X97-10102. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 1 (Thursday, January 2, 1997)]
    [Notices]
    [Pages 121-136]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X97-10102]
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from December 9, 1996, through December 19, 1996. 
    The last biweekly notice was published on December 18, 1996.
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the
    
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    proposed amendment would not (1) involve a significant increase in the 
    probability or consequences of an accident previously evaluated; or (2) 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated; or (3) involve a significant reduction 
    in a margin of safety. The basis for this proposed determination for 
    each amendment request is shown below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By February 3, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and
    
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    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-0001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: November 6, 1996
        Description of amendments request: The proposed amendment would 
    modify the technical specifications (TS) to require manual blocking of 
    one train of fast bus transfer (FBT) within the first hour of degraded 
    switchyard voltage should the switchyard voltage fall below the level 
    necessary for the electrical distribution system (EDS) degraded voltage 
    protection to maintain compliance with General Design Criteria (GDC) 
    17. The proposed amendment would further require the starting, 
    paralleling with the grid, loading, and then separating from the grid 
    the other train's emergency diesel generator (EDG) within the first 
    hour, rather than the current TS which allows two hours after onset of 
    a degraded switchyard voltage condition to start the EDG. 
    Alternatively, fast bus transfer can be blocked in both trains within 
    the first hour. The proposed amendment includes changes to the 
    applicable notes to reflect that these changes are no longer temporary, 
    but will remain as part of the long-term solution to this issue.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee provided 
    its analysis of the issue of no significant hazards consideration. The 
    NRC staff's analysis is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change reduces the amount of time the second train of 
    electrical equipment is allowed to remain in nonconformance with GDC 17 
    in the TS action statement. This change only affects equipment used to 
    mitigate an event, and does not affect equipment assumed to initiate 
    any event. Thus the probability of an accident previously evaluated is 
    not affected.
        The proposed change brings the second EDS train into compliance 
    with GDC 17 at least one hour sooner than the current TS. Once in 
    conformance with GDC 17, the consequences of accidents previously 
    evaluated conform to the current analysis. Thus the proposed change 
    does not increase the consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change only affects equipment designed to mitigate the 
    effects of an accident. The proposed change ensures that safety 
    equipment is configured as assumed in the current accident analysis. 
    The proposed change does not affect the conditions of structures, 
    systems, or components assumed in the safety analysis beyond the 
    existing design basis as maintained by the current TS. The proposed 
    change does not, therefore, create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The margin of safety affected by the proposed change is based on 
    calculated offsite dose consequences for postulated transients and 
    accidents for which the EDS provides power for equipment required to 
    mitigate. The proposed change reduces the time that one train of the 
    EDS is allowed to remain in nonconformance with GDC 17, thus 
    increasing the availability of the EDS prior to the onset of a 
    postulated accident compared to the current TS. Thus the proposed 
    change does not increase thecalculated offsite dose, and therefore 
    the proposed change does not involve a significant reduction in a 
    margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendments request involve no significant hazards 
    consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: November 26, 1996
        Description of amendments request: The proposed amendment will 
    adopt Option B of 10 CFR Part 50, Appendix J, to require Type B and 
    Type C containment leakage rate testing to be performed on a 
    performance-based testing schedule. Containment leakage rate testing is 
    currently performed in accordance with 10 CFR Part 50, Appendix J, 
    Option A, ``Primary Reactor Containment Leakage Testing for Water-
    Cooled Power Reactors.'' Appendix J specifies containment leakage 
    testing requirements, including the types of tests required, frequency 
    of testing, and reporting requirements. Containment leakage test 
    requirements include performance of Integrated Leakage Rate Tests, also 
    known as Type A tests, which measure overall leakage rate of the 
    containment; and Local Leakage Rate Tests, also known as Types B and C 
    tests, which measure the leakage through containment penetrations and 
    valves. The Nuclear Regulatory Commission (NRC) has amended the 
    regulations to provide an alternate performance-based option, Option B, 
    to the existing Appendix J. Baltimore Gas and Electric Company (BGE) 
    received approval to adopt Option B for Type A testing only. At this 
    time, BGE plans to adopt Option B for Types B and C testing, as well.
        BGE is revising the Containment Leakage Rate Testing Program for 
    Type A testing to implement Types B and C testing of the containment as 
    required by 10 CFR 50.54(o) and 10 CFR Part 50, Appendix J, Option B. 
    The revised program will be developed in accordance with the guidelines 
    contained in Regulatory Guide 1.163 ``Performance-Based Containment 
    Leak-Rate Test Program,'' dated September 1995, including errata.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
    
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        Containment leakage rate testing is performed in accordance with 
    10 CFR Part 50, Appendix J, ``Primary Reactor Containment Leakage 
    Testing for Water-Cooled Power Reactors.'' The Appendix J 
    containment leakage test requirements include performance of Type A 
    tests, which measure the overall leakage rate of the containment, 
    and Types B and C tests, which measure the leakage through 
    containment penetrations and valves. The Nuclear Regulatory 
    Commission has amended the regulations to provide a performance-
    based alternative, Option B, to the existing Appendix J. Baltimore 
    Gas and Electric Company adopted Option B for Type A testing during 
    the Unit 1 refueling outage earlier this year. At this time, BGE 
    plans to adopt Option B for Types B and C testing.
        Implementation of Option B involves no physical or operational 
    changes to the plant structures, systems, or components. 
    Furthermore, leakage rate does not contribute to the initiation of 
    any postulated accidents; therefore, this proposed change does not 
    involve an increase in the probability of any previously evaluated 
    accidents.
        Types B and C testing is necessary to demonstrate that leakage 
    through the containment penetrations is within the limits assumed in 
    the accident analyses. The only potential effect of the proposed 
    change to the Types B and C test frequency is the possibility that 
    containment penetration leakage would go undetected between tests. 
    To provide assurance that containment penetration leakage remains 
    within the limits of the Technical Specifications, BGE plans to 
    implement the performance-based leakage testing program in 
    accordance with NRC Regulatory Guide 1.163, dated September 1995 
    (including errata), with no exceptions.
        By adopting Option B, BGE will no longer require an exemption 
    from 10 CFR Part 50, Appendix J, which was granted to accommodate 
    24-month operating cycles. The exemption increased the surveillance 
    interval to a maximum of 30 months, while proportionately decreasing 
    the combined Types B and C leakage rate acceptance criteria. Option 
    B to Appendix J provides the regulation necessary to accommodate an 
    extended fuel cycle, while maintaining the original combined Types B 
    and C leakage rate testing limit. Therefore, BGE has requested 
    revocation of the exemption to 10 CFR Part 50, Appendix J, as 
    adoption of Option B for Types B and C testing will enable a return 
    to full compliance with Appendix J. As the facility will be in full 
    compliance with the regulations, this change does not increase the 
    consequences of any previously evaluated accidents.
        Implementation of Option B does not change the total allowable 
    containment leakage rate acceptance criteria, nor does it change the 
    total leakage assumed in the accident analyses. Option B allows the 
    implementation of a performance-based testing program to ensure that 
    resources are concentrated on the components most likely to exceed 
    administrative limits. Similarly, the changes to relocate the 
    procedural details, including test frequency, performance and data 
    conversion methodology, for containment leakage rate testing from 
    the Technical Specifications to the Containment Leakage Rate Testing 
    Program will have no effect on the total containment leakage allowed 
    by the Technical Specifications, or assumed in the accident 
    analyses. Relocating the allowable leakage rate conversions 
    (Standard Cubic Centimeters per Minute) to the Technical 
    Specification Bases does not change the allowable leakage rates (as 
    a percentage of the containment air volume) specified in the 
    Technical Specifications. Furthermore, relocation of the 
    programmatic controls for Types B and C testing, including the 
    allowable leakage rates, to the Administrative Controls section of 
    the Technical Specifications ensures an adequate level of regulatory 
    control of these criteria is retained.
        Additionally, the Calvert Cliffs Individual Plant Examination 
    considered the effects associated with severe accidents which could 
    lead to containment failure. It was concluded that adopting a 
    performance-based testing interval will not significantly affect the 
    containment failure probabilities calculated for the Individual 
    Plant Examination. Altogether, adoption of a performance-based 
    testing frequency, as specified in 10 CFR Part 50, Appendix J, 
    Option B, will not significantly decrease the confidence in the 
    leak-tightness of the containment, including containment 
    penetrations. Therefore, this change will not result in a 
    significant increase in the probability of undetected containment 
    penetration leakage in excess of that allowed by the Containment 
    Leakage Rate Testing Program, or assumed in the accident analysis, 
    or in the consequences of an accident previously evaluated.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed Technical Specification change adopts a 
    performance-based approach to containment penetration leakage rate 
    testing. This change does not add any new equipment, modify any 
    interfaces with any existing equipment, or change the equipment's 
    function, or the method of operating the equipment. The proposed 
    change does not affect normal plant operations or configuration, nor 
    does it affect leakage rate test methods. As the proposed change 
    would not change the design, configuration or operation of the 
    plant, it could not cause containment penetration leakage rate 
    testing to become an accident initiator.
        Therefore, the proposed change does not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The purpose of the existing schedule for Types B and C tests is 
    to provide assurance, on a regular basis, that the release of 
    radioactive material will be restricted to those leak paths and 
    leakage rates assumed in the accident analyses. The margin of safety 
    associated with containment penetration leakage rates is not reduced 
    if containment leakage does not exceed the maximum allowable leakage 
    rate defined in the Technical Specifications. Implementation of 
    Option B does not change the total allowable containment leakage 
    rate acceptance criteria, nor does it change the total leakage 
    assumed in the accident analyses. Option B only allows the 
    implementation of a performance-based testing program to ensure that 
    resources are concentrated on the components most likely to exceed 
    administrative limits. Similarly, the changes to relocate the 
    procedural details for containment leakage rate testing from the 
    Technical Specifications to either the Containment Leakage Rate 
    Testing Program or the Technical Specification Bases will have no 
    effect on the total containment leakage allowed by the Technical 
    Specifications, or assumed in the accident analyses. Furthermore, 
    relocation of the programmatic controls for Types B and C testing, 
    including the allowable leakage rates, to the Administrative 
    Controls section of the Technical Specifications ensures that the 
    same regulatory control of these criteria is retained.
        Elimination of the exemption to Appendix J which reduced the 
    amount of combined Types B and C testing allowable leakage 
    redistributes that portion of the total containment leakage which 
    may be attributed to local leakage rate testing, but does not affect 
    the maximum allowable containment leakage rate, La. The 
    proposed change does not affect a safety limit, a Limiting Condition 
    for Operation, or the way in which the plant is operated.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: S. Singh Bajwa, Acting Director
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: December 2, 1996 (NRC-96-0134)
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3.1.4.3, Rod Block Monitor, and 
    Tables 3.3.6-1 and 4.3.6-1 in TS 3.3.6, Control Rod Block 
    Instrumentation, to expand the range of conditions under which the rod 
    block monitor must be operable. These changes are required to ensure 
    that all fuel limits are met for the core that has been loaded for 
    Cycle 6.
    
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        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes provide requirements that are more 
    restrictive than the existing requirements for operation of the 
    facility. These changes provide assurance that the Rod Block Monitor 
    system is operable when necessary to prevent or mitigate transients 
    that could potentially threaten the integrity of the fuel cladding. 
    There will be no adverse impact on the probability of any accident 
    previously evaluated since the change provides additional assurance 
    that fuel thermal and mechanical design bases will be satisfied and 
    has no effect on any accident initiating mechanism. The additional 
    restrictive conditions on plant operation also ensure that the 
    consequences of anticipated operational occurrences are no more 
    severe than the most limiting conditions using the current Technical 
    Specifications. Therefore these changes do not involve any increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed changes will not involve any physical changes to 
    plant systems, structures, or components (SSC). The changes in Rod 
    Block Monitor operability requirements are consistent with the 
    current safety analysis assumptions. These requirements provide 
    assurance that the Rod Block Monitor will be operable if necessary 
    to terminate a rod withdrawal error so that fuel thermal and 
    mechanical design limits are satisfied. The change does not cause a 
    physical change to the plant or introduce a new mode of operation. 
    Therefore, the proposed amendment will not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. These changes maintain current assumptions within the safety 
    analyses and design basis. The changes provide assurance that the 
    Rod Block Monitor will be operable if necessary to terminate a rod 
    withdrawal error so that fuel thermal and mechanical design limits 
    are satisfied. Therefore, these changes do not involve a reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226
        NRC Project Director: John N. Hannon
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 6, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications to permit an increase in the 
    allowable leak rate for the Main Steam Isolation Valves (MSIVs) and 
    delete the Penetration Valve Leakage Control System (PVLCS) and Main 
    Steam-Positive Leakage Control System (MS-PLCS) requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The operation of River Bend Station, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of any accident previously evaluated.
        The proposed amendment to delete Technical Specification 3.6.1.8 
    and 3.6.1.9 involves eliminating the PVLCS and MS-PLCS leakage 
    control requirements from the Technical Specifications. As described 
    in Sections 9.3 and 6.7 respectively, of the USAR [Updated Safety 
    Analysis Report], the PVLCS and MS-PLCS are manually initialed about 
    20 minutes following a design basis LOCA [Loss of Coolant Accident].
        Since the PVLCS and MS-PLCS are operated only after an accident 
    has occurred, this proposed amendment has no effect on the 
    probability of an accident.
        Since MSIV leakage and operation of the PVLCS and MS-PLCS are 
    included in the radiological analysis for the design basis LOCA as 
    described in Section 15.6.5 of the USAR, the proposed amendments 
    will not affect the precursors of other analyzed accidents. The 
    PVLCS and MS-PLCS are not initiators of any previously analyzed 
    accident. The proposed amendments result in acceptable radiological 
    consequences of the design basis LOCA previously evaluated in 
    Section 15.6.5 of the USAR.
        The proposed amendment to Technical Specification 3.6.1.3 does 
    not involve a change to structures, components or systems that would 
    affect the probability of an accident previously evaluated. A plant-
    specific radiological analysis has been performed to assess the 
    affects of the proposed increase to the allowable MSIV leak rate and 
    deletion of the PVLCS and MS-PLCS in terms of Control Room and off-
    site doses following a postulated design basis LOCA. This change 
    required a revision to the existing LOCA dose analysis due to the 
    potential leakage from the MSIVs and those valves served by the 
    PVLCS. Additional changes were also included in the revised dose 
    analysis to account for changes in regulatory guidance and dose 
    methodology. Leakage from the drywell to the atmosphere through the 
    PVLCS (secondary containment bypass valves) are both assumed to 
    begin at time zero. The model conservatively assumes that one 
    inboard MSIV fails open at time zero and the MSIVs associated with 
    the remaining three main steam lines are assumed to begin leakage at 
    2 hours with a total leak rate of 200 scfh for all four main steam 
    lines. The design basis leak rate of the primary containment 
    (excluding main steam lines and lines sealed by the PVLCS) is 0.26% 
    of the containment volume by weight per 24 hours for the duration of 
    the accident and is assumed to be released entirely to the 
    environment initially or the secondary containment later into the 
    accident. The leakage of 170,000 cc/hr (4298 sccm) at Pa 
    through the containment isolation valves served by the PVLCS is 
    considered as bypass leakage circumventing the secondary 
    containment. The on-site and off-site doses were determined using 
    the TRANSACT computer code which included the ICRP 30 dose 
    conversion factors. The total off-site and on-site LOCA doses for 
    both the airborne and liquid release pathways resulting from the 
    proposed change are bounded by the applicable regulatory limits.
        The analysis demonstrates that dose contributions from the 
    proposed combined MSIV leakage rate limit of 200 scfh and from the 
    proposed deletion of the PVLCS and MS-PLCS result in values bounded 
    by the applicable regulatory limits as compared to the LOCA doses 
    previously evaluated for the off-site and Control Room doses as 
    contained in 10CFR100 and 10CFR50, Appendix A (General Design 
    Criteria 19), respectively. The LOCA doses previously evaluated are 
    discussed in Section 15.6.5 of the USAR.
        The whole body (DDE [Deep Dose Equivalent]) doses at the Low 
    Population Zone (LPZ) is 2.82 Rem and the Control Room is 0.43 Rem. 
    These values are acceptable since the revised doses are bounded by 
    the Regulatory Guidelines (2.82 versus 25 Rem at the LPZ and 0.43 
    versus 5 Rem at the Control Room). The associated whole boy (DDE) 
    dose at the exclusion area boundary (EAB) is 4.69 Rem which also 
    remains bounded by the Regulatory Guideline of 25 Rem.
        The thyroid CEDE [Committed Effective Dose Equivalent] dose at 
    the LPZ is 62.58 Rem. This is acceptable since the revised dose of 
    62.58 Rem is significantly less than the Regulatory Guideline (300 
    Rem). The EAB thyroid CEDE dose is 37.53 Rem, whereas the Control 
    Room thyroid CEDE dose is 11.18 Rem. These values are also 
    acceptable since the revised doses are well within the Regulatory 
    Guidelines (37.53 versus 300 Rem at the EAB and 11.18 versus 30 Rem 
    at the Control Room). The Control Room beta (SDE [Shallow Dose 
    Equivalent]) dose is 9.15 Rem which also remains bounded by the 
    Regulatory Guideline of 30 Rem.
        In summary, the proposed changes do not result in an increase to 
    the radiological consequences of a LOCA previously evaluated in the 
    USAR. The revised LOCA doses are bounded by the Regulatory 
    Guidelines. The effectiveness of the proposed request even for 
    leakage rates greater than the
    
    [[Page 126]]
    
    proposed MSIV allowable leak rate ensures that off-site and Control 
    Room dose limits are not exceeded.
        There is no physical change to the ADS/SRVs [Automatic 
    Depressurization System/Safety Relief Valve]. The PVLCS accumulator 
    tanks remain the backup air supply to the ADS/SRV accumulators. A 
    qualified long-term backup air supply remains but is supplied from a 
    difference source. Therefore, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed change deletes the requirements for the LCS 
    [Leakage Control System] isolation valves which are non-PCIVs. These 
    valves are eliminated and will not be performing a safety function. 
    The LCS lines that are connected to the PCIVs and process piping 
    will be welded and/or capped closed to assure primary containment 
    integrity is maintained. The welding and post-weld examination 
    procedures will be in accordance with the American Society of 
    Mechanical Engineers (ASME) Code, Section XI requirements. These 
    welds and/or caps will be periodically tested as part of the primary 
    Containment Integrated Leak Rate Test (CILRT) program in accordance 
    with the requirements of 10CFR50, Appendix J. The proposed change 
    does not involve an increase in the probability of equipment 
    malfunction previously evaluated in the USAR. In fact, the proposed 
    change reduces the probability of equipment malfunction since, upon 
    implementation, RBS will be operated with fewer process line 
    isolation valves and associated support equipment subjected to 
    postulated failure. The affected LCS MOVs [Motor Operated Valves] 
    will be eliminated or retained as normal system isolation or 
    maintenance valves having no safety or leakage control function thus 
    requiring no bypassing of their thermal overloads. This proposed 
    change has no effect on the consequences of an accident previously 
    evaluated since the LCS lines will be welded and/or capped closed, 
    thus assuring that primary containment integrity, isolation and leak 
    test capability are not compromised.
        Therefore, as discussed above, the proposed changes do not 
    involve a significant increase in the probability or consequences of 
    any accident previously evaluated.
        (2) The operation of River Bend Station, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed amendment to Technical Specification 3.6.1.3 does 
    not create the possibility for a new or different kind of accident 
    from any accident previously evaluated. The BWROG (Boiling Water 
    Reactors Owners Group) evaluated MSIV leakage performance and 
    concluded that MSIV leakage rates up to 200 scfh will not inhibit 
    the capability and isolation performance of the valve to isolate the 
    primary containment. There is no new modification which could impact 
    the MSIV operability. The LOCA has been reanalyzed at the proposed 
    maximum combined leakage rate of 200 scfh. Therefore, the proposed 
    change does not create any new or different kind of accident from 
    any accident previously evaluated in the USAR.
        The proposed amendment to delete Technical Specification 3.6.1.8 
    and 3.6.1.9 does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated because the 
    removal of the PVLCS and MS-PLCS does not affect any of the 
    remaining systems at RBS [River Bend Station) and the LOCA has been 
    reanalyzed with LOCA doses resulting from the proposed change 
    remaining bounded by the applicable regulatory limits.
        The PVLCS and MS-PLCS are of low safety significance as 
    discussed in NUREG-1273, Technical Findings and Regulatory Analysis 
    for Generic Safety Issue II.E.4.3, ``Containment Integrity Check,'' 
    and NUREG/CR-3539, ``Impact of Containment Building Leakage on LWR 
    Accident Risk.''
        The proposed change to eliminate the LCS does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated because the removal of the LCS does not 
    adversely affect any of the remaining RBS systems or change system 
    inter-relationships. The associated proposed changes to delete the 
    LCS isolation valves does not create the possibility of a new or 
    different kind of accident. The affected LCS MOVs will be eliminated 
    or retained as normal system isolation or maintenance valves having 
    no safety or leakage control function thus requiring no bypassing of 
    their thermal overloads. The PVLCS and MS-PLCS connections to the 
    process piping will be welded and/or capped closed to assure that 
    primary containment integrity, isolation and leak testing capability 
    are not compromised, therefore eliminating the possibility for any 
    new or different kind of accident.
        Therefore, as discussed above, the proposed changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        (3) The operation of River Bend Station, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed amendment to Technical Specification 3.6.1.3 does 
    not involve a significant reduction in a margin of safety. The 
    allowable leak rate limit specified for the MSIVs is used to 
    quantify a maximum amount of bypass leakage assumed in the LOCA 
    radiological analysis. Results of the analysis demonstrate 
    calculated doses, assuming the two single active failures of one 
    MSIV to close and one diesel generator to respond are bounded by the 
    requirements of 10CFR100 for the off-site doses and 10CFR50, 
    Appendix A (General Design Criteria 19) for the Control Room doses. 
    The calculated whole body doses are significantly reduced at the 
    LPZ, the Control Room, and the EAB. The calculated thyroid dose is 
    significantly reduced at the LPZ, the Control Room, and the EAB.
        The proposed amendment to delete Technical Specification 3.6.1.8 
    and 3.6.1.9 for the PVLCS and MS-PLCS, does not reduce the margin of 
    safety. In fact, the overall margin of safety is increased. The 
    method is effective to reduce dose consequences of MSIV and the 
    PVLCS leakage over an expanded operating range and will, thereby, 
    resolve the safety concern that the PVLCS and MS-PLCS will not 
    function at leakage rates higher than their design capacity. The 
    method is consistent with the philosophy of protection by multiple 
    leak-tight barriers used in containment design for limiting fission 
    product release to the environment. Therefore, the proposed method 
    is highly reliable and effective for MSIV leakage and deletion of 
    the PVLCS and MS-PLCS.
        The calculation shows that MSIV leakage rates up to 100 scfh per 
    steam line would not exceed the regulatory limits. Therefore, the 
    proposed method provides a substantial safety margin for mitigating 
    the radiological consequences of MSIV leakage beyond the proposed 
    Technical Specification leak rate limit of 200 scfh for all four 
    main steam lines (combined maximum pathway).
        Minor increases in containment leakage such as the leakage 
    through the MSIVs, as identified in NUREG-1273, NUREG/CR-3539, and 
    NUREG-1493 have been found to have no significant impact on the risk 
    to the public. Therefore, the proposed change does not result in a 
    significant reduction in a margin of safety.
        The proposed change to delete the LCS isolation valves does not 
    reduce the margin of safety. Welded and/or capped closure of the LCS 
    lines assure that primary containment integrity and leak testing 
    capability are not compromised. The affected LCS MOVs will be 
    eliminated or retained as normal system isolation or maintenance 
    valves having no safety or leakage control function thus requiring 
    no bypassing of their thermal overloads. The PVLCS and MS-PLCS 
    connections to the process piping will be welded and/or capped 
    closed to assure that primary containment integrity, isolation and 
    leak testing capability are not compromised, therefore eliminating 
    the possibility for a significant reduction in the margin of safety.
        Therefore, as discussed above, the proposed changes do not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    [[Page 127]]
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 15, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications to allow the performance of the 24-
    hour emergency diesel generator (EDG) maintenance run while the unit is 
    in either Mode 1 or Mode 2. This test for the River Bend Station (RBS) 
    is currently prohibited in Mode 1 and Mode 2 and allowed in Modes 3, 4, 
    and 5.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The RBS SAR [Safety Analysis Report] assumes that the AC 
    [Alternating Current] electrical power sources are designed to 
    provide sufficient capacity, capability, redundancy and reliability 
    to ensure that the fuel, reactor coolant system and containment 
    design limits are not exceeded during an assumed design basis event. 
    Specifically, the SAR assumes that the onsite EDGs provide emergency 
    power in the event offsite power is lost to either one or all three 
    EDF [Engineered Safety Features]
        buses. In the event of a loss of preferred power, the ESF 
    electrical loads are automatically connected to the EDGs in 
    sufficient time to provide for safe reactor shutdown and to mitigate 
    the consequences of a design basis accident such as a LOCA [Loss of 
    Coolant Accident].
        The proposed change to permit the 24-hour testing of the EDGs 
    during power operation does not significantly increase the 
    probability or consequences of any previously evaluated accident. 
    The capability of the EDGs to supply power in a timely manner will 
    not be compromised by permitting performance of EDG testing during 
    periods of power operation. Design features of the EDGs and 
    electrical systems ensure that if a LOCA or LOP [Loss of Offsite 
    Power] signal, either individually or concurrently, should occur 
    during testing, the EDG would be returned to its ready-to-load 
    condition (i.e., EDG running at rated speed and voltage separated 
    from the offsite sources) or separately connected to the ESF bus 
    providing ESF loads. An EDG being tested is considered to be 
    operable and fully capable of meeting its intended design function. 
    Additionally, the testing of an EDG is not a precursor to any 
    preciously evaluated accidents.
        If, during the test period, the EDG were to receive a normal 
    operation protective trip resulting in the actuation of a generator 
    lockout signal, the lockout could be reset by the operators 
    monitoring the test. The resulting delay does not present an 
    immediate challenge to the fuel cladding integrity, reactor water 
    level control or to containment parameters, as demonstrated by the 
    bounding four-hour station blackout coping analysis contained in 
    RBS's station blackout conformance report.
        Therefore, the proposed change allowing testing of EDGs during 
    power operation will not significantly increase the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        As previously discussed, the proposed change to permit the 
    performance of EDG testing during power operation will not affect 
    the operation of any system or alter any system's response to 
    previously evaluated design basis events. The EDGs will 
    automatically transfer from the test configuration to the ready-to-
    load configuration following receipt of a valid signal (i.e., LOCA 
    or LOP). In the ready-to-load configuration the EDG will be running 
    at rated speed and voltage, separated from the offsite source and 
    capable of automatically supplying power to the ESF buses in the 
    event that preferred power is actually lost.
        The proposed change is also the same configuration currently 
    used for the monthly one-hour test. Therefore, testing during power 
    operation will not create the possibility of a new or different kind 
    of event from any previously evaluated.
        [Surveillance Requirement] SR 3.8.1.16 demonstrated that the EDG 
    will automatically override the test mode following generation of a 
    LOCA signal. In addition, the ability of the EDGs to survive a full 
    load reject is verified by the performance of SR 3.8.1.9. These 
    existing surveillance requirements, along with system design 
    features, ensure that the performance of EDG testing during power 
    operation will not create the possibility of a new or different kind 
    of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The AC electrical power sources are designed to provide 
    sufficient capacity, capability, redundancy, and reliability to 
    ensure the availability of necessary power to ESF systems so that 
    the fuel, reactor coolant system and containment design limits are 
    not exceeded. Specifically, the EDGs must be capable of 
    automatically providing power to ESF loads in sufficient time to 
    provide for safe reactor shutdown and to mitigate the consequences 
    of a design basis accident in the event of a loss of preferred 
    power.
        Testing of EDGs during power operation will not affect the 
    availability or operation of any offsite source of power. In 
    addition, the EDG being tested remains capable of meeting it 
    intended design functions. Therefore, the proposed change to the 
    Technical Specification Surveillance Requirement 3.8.1.13 will not 
    result in a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 15, 1996
        Description of amendment request: The proposed amendment would 
    increase the two recirculation loop Minimum Critical Power Ratio (MCPR) 
    limit from 1.07 to 1.10 and the single recirculation loop MCPR limit 
    from 1.08 to 1.12. This change request is the result of a non-
    conservative calculation identified by the fuel vendor.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The request does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The revised Safety Limit MCPR and the cycle-specific thermal 
    limits that are based on the revised SLMCPR have been calculated 
    using the methods identified in the ``Supplemental Reload Licensing 
    Report For River Bend Station Reload 6 Cycle 7'' (Reference 1). 
    These methods are within the existing design and licensing basis and 
    cannot increase the probability or severity of an accident. The 
    basis of the MCPR Safety Limit calculation is to ensure that greater 
    that [than] 99.9% of all fuel rods in the core avoid transition 
    boiling and fuel damage in the event of a postulated accident.
        The SLMCPR is used to establish the Operating Limit Minimum 
    Critical Power Ratio (OLMCPR). Neither the SLMCPR nor the OLMCPR can 
    initiate an event, therefore[,] a change to the SLMCPR does not 
    increase the probability of a accident previously evaluated. 
    Maintaining the Minimum Critical Power Ratio (MCPR) at or above the 
    OLMCPR during normal operations precludes fuel failure due to 
    overheating of the fuel clad during an anticipated operational 
    occurrence (AOO), thus limiting the consequences of an AOO. The 
    proposed change will increase the SLMCPR, which will require the 
    OLMCPR to be increased,
    
    [[Page 128]]
    
    which in turn will ensure that the requirements of 10 CFR [Part] 100 
    are met for an AOO. Therefore, there is no increase in the 
    consequences of an accident previously analyzed.
        The request does not create the possibility of occurrence of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The MCPR Safety Limit is a Technical Specification numerical 
    value designed to ensure that fuel damage from transition boiling 
    does not occur as a result of the limiting postulated accident. It 
    cannot create the possibility of any new type of accident.
        Neither the SLMCPR or the OLMCPR can initiate an event, 
    therefore, a change to the SLMCPR does not create the possibility of 
    occurrence of a new or different kind of accident from any accident 
    previously evaluated.
        The request does not involve a significant reduction in the 
    margin of safety.
        The MCPR Safety Limit is a Technical Specification numerical 
    value designed to ensure that fuel damage from transition boiling 
    does not occur as a result of the limiting postulated accident. This 
    new Safety Limit MCPR is calculated using the methods identified in 
    the reference. These methods are within the existing design and 
    licensing basis and based on RBS specific inputs.
        The margin of Safety resides between the SLMCPR and the point at 
    which fuel fails. The proposed change to SLMCPR (and the OLMCPR) 
    will in fact restore the margin of safety associated with GE's 
    SLMCPR methodology.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
        Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
        Date of amendment request: December 2, 1996
        Description of amendment request: The proposed Technical 
    Specification (TS) Change Request will permit the use of 10CFR50 
    Appendix J, Option B, Performance-Based Containment Leakage Testing for 
    Type A, B and C leak rate testing. TSs 3/4.6.1.1, 3/4.6.1.2, 3/4.6.1.3, 
    4.6.1.6 and 4.6.1.7 are revised and Section 6.15 is added establishing 
    the Containment Leakage Rate Testing Program. The Bases are revised to 
    reflect this change. Minor editorial changes are included in this 
    request. Waterford Steam Electric Station is planning to have a 
    Containment Leakage Rate Testing Program in place prior to the next 
    scheduled refueling outage. This program will be in accordance with the 
    guidelines contained in Regulatory Guide 1.163, ``Performance-Based 
    Containment Leak-Test Program,'' dated September 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change will not affect the assumptions, design 
    parameters, or results of any accident previously evaluated. The 
    proposed change does not add or modify any existing equipment. The 
    proposed changes will result in increased intervals between 
    containment leakage tests determined through a performance based 
    approach. The intervals between such tests are not related to 
    conditions which cause accidents. The proposed changes do not 
    involve a change to the plant design or operation. Therefore, this 
    change does not involve a significant increase in the probability of 
    any accident previously evaluated.
        NUREG-1493, ``Performance-Based Containment Leak-Test Program,'' 
    contributed to the technical bases for Option B of 10 CFR 50 
    Appendix J. NUREG-1493 contains a detailed evaluation of the 
    expected leakage from containment and the associated consequences. 
    The increased risk due to lengthening of the intervals between 
    containment leakage tests was also evaluated and found acceptable. 
    Using a statistical approach, NUREG-1493 determined the increase in 
    the expected dose to the public from extending the testing frequency 
    is extremely small. It also concluded that a small increase is 
    justifiable due to the benefits which accrue from the interval 
    extension. The primary benefit is in the reduction in occupational 
    exposure. The reduction in the occupational exposure is a real 
    reduction, while the small increase to the public is statistically 
    derived using conservative assumptions. Therefore, this change does 
    not involve a significant increase in the consequences of any 
    accident previously evaluated.
        The proposed change does not involve modifications to any 
    existing equipment. The proposed change will not affect the 
    operation of the plant or the manner in which the plant is operated. 
    The reduced testing frequency will not affect the testing 
    methodology. Therefore, the proposed change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed change does not change the performance methodology 
    of the containment leakage rate testing program. However, the 
    proposed change does affect the frequency of containment leakage 
    rate testing. With an increased frequency between tests, the 
    proposed change does increase the probability that a increase in 
    leakage could go undetected for a longer period of time. Operational 
    experience has demonstrated the leak tightness of the containment 
    buildings has been significantly below the allowable leakage limit.
        The margin of safety that has the potential of being impacted by 
    the proposed change involves the offsite dose consequences of 
    postulated accidents which are directly related to containment 
    leakage rates. The limitation on containment leakage rate is 
    designed to ensure the total leakage volume will not exceed the 
    value assumed in our accident analysis. The margin of safety for the 
    offsite dose consequences of postulated accidents directly related 
    to containment leakage is maintained by meeting the 1.0 La 
    acceptance criteria. The proposed change maintains the 1.0 La 
    acceptance criteria. Therefore, the proposed change will not involve 
    a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of amendment request: September 19, 1996
        Description of amendment request: The proposed changes to Plant 
    Hatch Units 1 and 2 Technical Specifications would revise the 
    Surveillance Requirements (SRs) addressing the reactor vessel pressure 
    and temperature (P/T) limits. The affected SRs are 3.4.9.1, 3.4.9.2, 
    3.4.9.3, 3.4.9.4, 3.4.9.5, 3.4.9.6, and 3.4.9.7, and the corresponding 
    Units 1 and 2 Figures 3.4.9-1, 3.4.9-2, and 3.4.9-3, which show P/T 
    limit curves for inservice leak and hydrostatic testing, non-nuclear 
    heatup and cooldown, and criticality, respectively.
        The P/T curves would be changed to allow separate monitoring of the 
    three major regions of the reactor pressure vessel (RPV) (i.e., the 
    upper vessel and flange region, the beltline region, and the bottom 
    head region), and to extend the validity of the Unit 1 curves to 32
    
    [[Page 129]]
    
    Effective Full Power Years (EFPY). Separate monitoring would alleviate 
    the difficulties with meeting certain temperature requirements due to 
    the artificial limits imposed by the current P/T curves.
        In support of the proposed changes, General Electric (GE) prepared 
    and issued GENE-523-A137-1295, ``E. I. Hatch Nuclear Power Station, P-T 
    Curve Modification for Unit 1 and Unit 2,'' which is provided in the 
    submittal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Pressure and temperature (P/T) limits for the reactor pressure 
    vessel (RPV) are established to ensure brittle fracture of the 
    vessel does not occur.
        A. The proposed changes merely clarify the Applicability of the 
    P/T limits for each of the low pressure conditions by replacing the 
    word ``performed'' with ``met'', adding Notes to Surveillance 
    Requirements, incorporating the requirements of Notes into the 
    Surveillance Requirements, and modifying the Frequency statements. 
    Conditions 2, 3, and 4, discussed in Enclosure 1 ``justification of 
    changes'', [of the licensee's application] have their own 
    Surveillance Requirements. Temperature requirements for Condition 1 
    are specified in the Bases. This proposed change only clarifies 
    which Surveillance Requirement applies to each operating 
    configuration. No reduction in Surveillance Frequencies is proposed.
        B. The proposed revisions to the operating limits curves for 
    inservice leak and hydrostatic testing, and the heatup and cooldown 
    allow independent monitoring of the three RPV regions; i.e., the 
    bottom head, the upper vessel and flange, and the core beltline. The 
    three Unit 1 curves, including the criticality curve, were extended 
    to 32 Effective Full Power Years (EFPY), and a correction to the 
    Unit 1 criticality curve was made. Operating limits for each of the 
    curves were evaluated in accordance with the methodology given in 
    the applicable ASME Codes; Regulatory Guide 1.99, Rev. 2, and 
    Appendix G of 10 CFR [Part] 50.
        The actual limits in the inservice leak and hydrostatic testing 
    curves, and the heatup and cooldown curves were not relaxed. 
    Therefore, segregating the curves into the three affected vessel 
    regions does not represent a reduction in the actual P/T 
    requirements. The current P/T curves represent a composite of the 
    three regions, with each point representing the limiting region. 
    Regions of the vessel that are not limiting at a specific point are, 
    therefore, artificially restrained. Upon implementation of the 
    proposed changes, each vessel region will have its own curve, with 
    its own true limit.
        Since the proposed changes do not affect the recirculation 
    piping, the probability and the consequences of a loss of coolant 
    accident are not increased. Likewise, no other previously evaluated 
    accidents or transients, as defined in Chapters 14 and 15 of the 
    Units 1 and 2 Final Safety Analysis Reports, are affected by the 
    proposed changes.
        In summary, the proposed changes do not represent a relaxation 
    of any actual operating limit and do not reduce the Frequency of any 
    Surveillance. Three of the four operating configurations of the RPV 
    are covered by Surveillance Requirements. Temperature limitations 
    for the head removed from the vessel are given in the Bases. The 
    operating limits were developed using the approved methodology 
    contained in 10 CFR [Part] 50, Appendix G. Therefore, the 
    probability and consequences of a brittle fracture of the RPV are 
    not increased.
        2. Do the proposed changes create the possibility of a new or 
    different type of accident from any previously evaluated.
        Implementing the low pressure changes, or the new operating 
    limit curves, does not alter the design or operation of any system 
    designed for the prevention or mitigation of accidents. The proposed 
    changes do not introduce any new type of normal or abnormal 
    operating mode or failure mode. All P/T limits for the Unit 1 and 
    the Unit 2 reactor vessels continue to be monitored per the 
    requirements of 10 CFR [Part] 50, Appendices G and H. Therefore, the 
    proposed changes do not create the possibility of a new type of 
    accident.
        3. Do the proposed changes involve a significant reduction in 
    the margin of safety?
        The purpose of the P/T limits is to ensure a brittle fracture of 
    the RPV does not occur. The proposed Technical Specifications 
    changes for the low pressure conditions are made for clarification 
    purposes. No operating limits or Surveillance Requirements are 
    relaxed. The wording of current Technical
        Specifications SRs 3.4.9.1, 3.4.9.2, 3.4.9.5, 3.4.9.6, and 
    3.4.9.7 could result in overly conservative application of the 
    requirements. The proposed amendment is written to remove the 
    ambiguity in that the Applicability and Frequency of each 
    Surveillance Requirement are clear. Neither the acceptance criteria 
    nor the Surveillance Frequency of any Surveillance is reduced. 
    Furthermore, the four possible RPV configurations are all adequately 
    monitored. As a result, the margin of safety for the low pressure 
    conditions is not significantly reduced due to the proposed changes.
        The Unit 1 operating curves were extended to 32 EFPY using 
    approved methodologies. More operational margin is provided, because 
    the three vessel regions (upper vessel and flange, beltline, and 
    bottom head) are being separated for the inservice leak and 
    hydrostatic testing curve, and the heatup and cooldown curve. 
    Although this separation results in more operating margin for 
    certain vessel regions, it does not represent a significant 
    reduction in the margin of safety. As described previously, the 
    current Technical Specifications curves represent a composite of the 
    three regions. Thus, the curves represent the temperature for the 
    limiting region at a particular point. The regions that are not 
    limiting at a particular point are artificially restricted. 
    Separating the three regions, as proposed, eliminates false limits. 
    The true limit for each region is preserved and uncompromised, based 
    on the use of approved methodologies.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of amendment request: October 7, 1996
        Description of amendment request: The proposed changes to Plant 
    Hatch Unit 1 and Unit 2 Technical Specifications (TS) would revise 
    Surveillance Requirements (SR) 3.1.7.7 and 3.4.3.1, and Limiting 
    Conditions for Operation (LCO) 3.4.3, 3.5.1, and 3.6.1.6, to increase 
    the nominal mechanical pressure relief setpoints for all of the 11 
    safety/relief valves (SRV) to 1150 psig and allow operation with one 
    SRV and its associated functions inoperable. The proposed changes would 
    reduce the potential for SRV pilot leakage and the potential for forced 
    outages due to an inoperable SRV during a fuel cycle.
        The existing TS require that during continuous operation, all of 
    the 11 SRVs remain OPERABLE in the safety mode, 7 in the Automatic 
    Depressurization System (ADS) mode, and 4 in the Low-Low Set (LLS) 
    mode. If one SRV is inoperable for longer than the duration specified 
    in the applicable Action Statements, the plant must be placed in a Cold 
    Shutdown Condition. Analyses have been completed which show that, with 
    one SRV out of service, all transient/accident criteria can still be 
    met. Increasing the nominal mechanical relief setpoints will increase 
    the simmer margin (i.e., the difference between the SRV setpoints and 
    the vessel steam dome pressure), thereby potentially reducing SRV pilot 
    leakage which may occur during a typical operating cycle.
    
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    As a result of increasing the mechanical relief setpoints for the SRVs, 
    the Standby Liquid Control (SLC) System pump test discharge pressure is 
    increased to 1232 psig. The High Pressure Coolant Injection (HPCI) and 
    Reactor Core Isolation Cooling (RCIC) systems are capable of operating 
    at this increased pressure.
        In support of the proposed changes, General Electric (GE) prepared 
    NEDC-32041P, ``Safety Review for Edwin I. Hatch Nuclear Power Plant 
    Units 1 and 2 Updated Safety/Relief Valve Performance Requirements,'' 
    Revision 2, dated April 1996, which was included in the submittal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The SRVs serve to mitigate postulated transients and accidents; 
    the proposed changes do not alter the function or mode of operation 
    of the SRVs. The probability of an OPERABLE or an INOPERABLE SRV 
    inadvertently opening or failing to open or close is not affected by 
    these changes. Therefore, the probability of an accident is not 
    increased. Analysis(a) has been performed which considers the 
    consequences of the various transients and accidents with the 
    increased setpoints and with one SRV inoperable. The analysis also 
    considers the impact on ECCS [Emergency Core Cooling System] 
    performance, including HPCI and RCIC. The analysis has shown that 
    the consequences of an accident with the increased SRV setpoints and 
    with one SRV inoperable are not increased.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        Revising the nominal SRV setpoint only changes when the SRV 
    opens in its mechanical relief mode; the operation of the SRV and 
    any other existing equipment is not altered. Operation with one SRV 
    inoperable was evaluated(a) and does not introduce any new 
    failure modes. The impact on the operation and design of other 
    systems and components has been evaluated,(a) including ECCS 
    and SLC. No new operating modes or failure modes are introduced. 
    Thus, these changes do not contribute to a new or different type of 
    accident.
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety.
        The change in SRV setpoint and operation with one SRV inoperable 
    was evaluated relative to the applicable safety system settings and 
    found to remain acceptable. For example, the proposed changes were 
    evaluated against peak clad temperature limits, ECCS operation, ASME 
    Code overpressurization limits, the MINIMUM CRITICAL POWER RATIO 
    Safety Limit, and containment design limits; no significant 
    reduction in the margin of safety was identified(a).
        (a) GE Report NEDC-32041P, ``Safety Review for Edwin I. Hatch 
    Nuclear Power Plant Units 1 and 2 Updated Safety/Relief Valve 
    Performance Requirements, Revision 2 (Proprietary), April 1996''.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of amendment request: October 29, 1996
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications (TS) for Plant Hatch Units 1 and 2 
    associated with the installation of a digital Power Range Neutron 
    Monitoring (PRNM) system and the incorporation of long-term stability 
    solution hardware.
        In response to Generic Letter 94-02, ``Thermal-Hydraulic 
    Instabilities in Boiling Water Reactors,'' Georgia Power Company (GPC) 
    selected General Electric (GE) Option III as the long-term stability 
    solution. Option III detects core instabilities and provides a reactor 
    scram signal to the Reactor Protection System (RPS). The long-term 
    stability solution, GE Option III, is supported by the BWR Owners' 
    Group Topical Report NEDO-31960-A submitted to the NRC for approval in 
    May 1991, and NEDO-31960-A, Supplement 1, submitted to the NRC for 
    approval in March 1992. The NRC issued a Safety Evaluation Report (SER) 
    for NEDO-31960-A and Supplement 1 in July 1993. BWR Owners' Group 
    Topical Report NEDO-32465, submitted to the NRC in June 1995, provides 
    additional analysis for the detection and suppression methodology 
    (Option III).
        To execute the stability solution software, the Average Power Range 
    Monitor (APRM) and Rod Block Monitor (RBM) electronics would be 
    replaced with a PRNM system based on digital GE Nuclear Measurements 
    Analysis and Control NUMAC modules. Implementation of the PRNM would 
    affect the RPS and Control Rod Block TS 3.3.1.1, 3.3.2.1, 3.4.1 and 
    3.10.8.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The purpose of the proposed amendment is to incorporate the 
    Power Range Neutron Monitoring (PRNM) retrofit and Oscillation Power 
    Range Monitor (OPRM) installation. The types of Average Power Range 
    Monitor (APRM) Functions that are credited to mitigate accidents 
    were previously evaluated. The proposed OPRM Upscale Function is 
    implemented in the same hardware that implements the APRM Functions. 
    The change to a two-out-of-four RPS [Reactor Protection System] 
    logic was analyzed and determined to be equal to the original logic.
        The modification involves equipment that is intended to detect 
    the symptoms of some accidents and initiate mitigating action. The 
    worst case failure of the equipment involved in the modification is 
    a failure to initiate mitigating action (scram), but no failure can 
    cause an accident. As discussed in the bases for proposed changes, 
    the PRNM replacement system is designed to perform the same 
    operations as the existing Power Range Monitoring (PRM) system and 
    to meet or exceed all of its operational requirements. Therefore, it 
    is concluded that the probability of an accident previously 
    evaluated is not increased as a result of replacing the existing 
    equipment with the PRNM equipment.
        * * * *
        Human-machine interface (HMI) failures in the current system 
    could be related to incorrectly adjusted settings, incorrect reading 
    of meters, and failure to return the equipment to the normal 
    operating configuration. There are comparable failure modes for some 
    of these problems in the digital system where an erroneous 
    potentiometer adjustment in the current system is equivalent to an 
    erroneous digital entry in the replacement system. Certain potential 
    ``failure to reconfigure errors'' in the current system have no 
    counterpart in the replacement system, because any reconfiguration'' 
    is automatically returned to normal by the system. Also, since 
    parameters are available for review at any time, even if an error, 
    such as a digital entry error occurs, it is more likely that the 
    error would be almost immediately detected by recognition that the 
    displayed value is not the correct one.
        The failure analysis of the current system assumes certain rates 
    of human error. The rates for the replacement system will be lower 
    and, hence, are bounded by the FSAR [Final Safety Analysis Report] 
    analysis.
        Therefore, GPC [Georgia Power Company] concludes the proposed 
    changes do not
    
    [[Page 131]]
    
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The APRM Trip Functions credited in the accident analyses are 
    retained in the PRNM retrofit. The response time of the new 
    electronics meets or exceeds the required response criteria. No new 
    interfaces or interactions with other equipment will introduce any 
    new failure modes.
        The modification involves equipment that is intended to detect 
    the symptoms of some accidents and initiate mitigating action. The 
    worst-case failure of the equipment involved in the modification is 
    a failure to initiate mitigating action (scram), but no failure can 
    cause an accident. This is unchanged from the current system.
        Software common-cause failures can at most cause the system to 
    fail to perform its safety function. In that case, it could fail to 
    initiate action to mitigate the consequences of an accident, but 
    would not cause one.
        The new system is a digital system with software (firmware) 
    control. As such, it has ``central'' processing points and software 
    controlled digital processing where the current system had analog 
    and discrete component processing. The result is that the specific 
    failures of hardware and potentially common-cause software failures 
    are different from the current system. Also, automatic self-test 
    results in some cases in a direct trip as a result of a hardware 
    failure where the current system may have remained ``as-is''. 
    However, when these are evaluated at the system level, there are no 
    new effects. In general, FSARs assume simplistic failure modes 
    (relays for example) but do not specifically evaluate such effects 
    as self-test detection and automatic trip or alarm.
        The effects of software common-cause failure are mitigated by 
    hardware design and system architecture. The replacement equipment 
    is fully qualified to operate in its installed location and will not 
    affect other equipment.
        Therefore, GPC concludes the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The replacement equipment provides the same function as the 
    original electronics. Response time and operator information are 
    either maintained or improved. The equipment was qualified, where 
    appropriate, to assure its intended safety function is performed. 
    The replacement system has improved channel trip accuracy compared 
    to the current system and meets or exceeds system requirements 
    assumed in setpoint analysis. The channel response time exceeds the 
    requirements. The channel indicated accuracy is improved over the 
    current system, and meets or exceeds system requirements. The 
    replacement system meets or exceeds all system requirements.
        The BWROG [BWR Owners' Group] Stability Option III was developed 
    to meet the requirements of GDC [General Design Criterion] 10 and 
    GDC 12 by providing a hardware system that detects the presence of 
    thermal-hydraulic instabilities and automatically initiates the 
    necessary actions to suppress the oscillations prior to violating 
    the MCPR [maximum critical power ratio] Safety Limit. The NRC has 
    reviewed and accepted the Option III methodology described in 
    Licensing Topical Report NEDO-31960 and concluded this solution will 
    provide the intended protection. Therefore, it is concluded that 
    there will be no reduction in the margin of safety as defined in the 
    Technical Specifications as a result of the installation of the OPRM 
    system and the simultaneous removal of the operating restrictions 
    imposed by the ICAs [item control areas].
        Therefore, GPC concludes the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: November 20, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to allow the Vice President to 
    designate the Safety Audit and Review Committee (SARC) Chairperson, to 
    change the work hours limitation in accordance with guidance in GL 82-
    12, ``Nuclear Power Plant Staff Working Hours;'' to change radioactive 
    shipments record retention requirements to comply with recent 10 CFR 
    Part 20 changes; and other editorial changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The changes requested are administrative in nature. Paragraph 
    3.D was placed in the License by Amendment No. 155 to authorize 
    Omaha Public Power District (OPPD) to increase the storage capacity 
    of the FCS spent fuel pool. Amendment No. 155 stated that the TS as 
    issued would be effective when the last new rack was installed. 
    Since the last new rack was installed on
    
        August 8, 1994, Paragraph 3.D is no longer necessary and should
    
        be deleted from the License.
        Table of Contents, Section 6.0, ``Interim Special Technical 
    Specifications,'' Subsections 6.1 through 6.4 are proposed for 
    deletion because all of the Specifications referred to have been 
    deleted by previous Amendments.
        The revision proposed for TS 2.15 (Item 2C of Table 2-3 & Item 
    1C of Table 2-4) will insert the correct terminology (Pressurizer 
    Low/Low Pressure) into the Functional Unit description.
        The revision proposed for TS 5.2 will require the control of 
    overtime worked by personnel to be in accordance with the NRC Policy 
    Statement on working hours (Generic Letter 82-12) in lieu of stating 
    the specific times requirements from the Policy as the current TS 
    does. This option is in accordance with NUREG-1432, Standard TS for 
    Combustion Engineering Plants, Specification 5.2.2e, and will allow 
    work groups to be on twelve hour shifts.
        The revision proposed for TS 5.5.2.2 will replace the specific 
    title of the Chairperson of the Safety Audit and Review Committee 
    and replace it with ``Member as appointed by the Vice President.'' 
    This will allow the flexibility to change chairmanship of the 
    committee amongst the members.
        The revision to TS 5.10 concerning retention of records of 
    radioactive shipments will update the TS to current 10 CFR 20 
    requirements. Plant procedures already comply with current 10 CFR 20 
    record retention requirements. The addition of the Section 5.0 title 
    corrects a minor format discrepancy.
        These proposed revisions are administrative in nature. The 
    proposed revisions have no effect on any initial assumptions or 
    operating restrictions assumed in any accident, nor do these changes 
    have any effect on equipment required to mitigate the consequences 
    of an accident. Therefore the proposed revisions do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed revisions correct minor errors, remove outdated 
    information, are consistent with changes in organizational 
    structure, 10 CFR Part 20, or NUREG-1432, ``Combustion Engineering 
    Standard Technical Specifications (STS). These changes will not 
    result in any physical alterations to the plant configuration, 
    changes to setpoint values, or changes to the application of 
    setpoints or limits. No new operating modes are proposed as a result 
    of these changes. Therefore the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
    
    [[Page 132]]
    
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The revisions listed above correct minor errors, remove outdated 
    information, or are consistent with changes in organizational 
    structure, 10 CFR Part 20, or Standard TS. These changes will not 
    result in any physical alterations to the plant configuration, 
    changes to setpoint values, or changes to the application of 
    setpoints or limits. Therefore the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William H. Bateman
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: October 28, 1996
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Section 3/4.8.1, ``A.C. Sources,'' 
    TS Section 3/4.8.2, ``Onsite Power Distribution Systems,'' TS Table 
    4.8.1, ``Battery Surveillance Requirements,'' and the associated bases. 
    Surveillance requirements would be modified to account for the increase 
    in the fuel cycle, consistent with Generic Letter 91-04, ``Changes in 
    Technical Specification Surveillance Intervals to Accommodate a 24-
    month Fuel Cycle,'' dated April 2, 1991. Administrative changes are 
    also proposed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Toledo Edison has reviewed the proposed changes and determined 
    that a significant hazards consideration does not exist because 
    operation of the Davis-Besse Nuclear Power Station, Unit No. 1, in 
    accordance with these changes would:
        1a. Not involve a significant increase in the probability of an 
    accident previously evaluated because no such accidents are affected 
    by the proposed revisions to increase the surveillance test 
    intervals from 18 to 24 months for the A.C. Offsite Sources, the 
    Emergency Diesel Generators and the Station Batteries or the 
    proposed revision to remove the ``during shutdown'' restriction for 
    conduct of the battery performance test.
        Results of the review of historical 18 month surveillance data 
    and maintenance records support an increase in the surveillance test 
    intervals from 18 to 24 months (and up to 30 months on a non-routine 
    basis) because no potential for a significant increase in a failure 
    rate of a system or component was identified during these reviews.
        These proposed revisions are consistent with the NRC guidance on 
    evaluating and proposing such revisions as provided in Generic 
    Letter 91-04, ``Changes in Technical Specification Surveillance 
    Intervals to Accommodate a 24-Month Fuel Cycle,'' dated April 2, 
    1991.
        Initiating conditions and assumptions remain as previously 
    analyzed for accidents in the DBNPS Updated Safety Analysis Report.
        These revisions do not involve any physical changes to systems 
    or components, nor do they alter the typical manner in which the 
    systems or components are operated.
        The proposed revision to reflect that the battery charger 
    performance test will continue to be conducted on a[n] 18 month 
    surveillance interval is an administrative change and does not 
    affect previously analyzed accidents.
        The proposed revision to the Bases to reflect that a change to a 
    24 month surveillance test interval is an exception to current 
    guidance is an administrative change and does not affect previously 
    analyzed accidents.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because the source term, containment 
    isolation or radiological releases are not being changed by these 
    proposed revisions. Existing system and component redundancy is not 
    being changed by these proposed changes. Existing system and 
    component operation is not being changed by these proposed changes 
    and the assumptions used in evaluating the radiological consequences 
    in the DBNPS Updated Safety Analysis Report are not invalidated.
        2. Not create the possibility of a new or different kind of 
    accident from any accident previously evaluated because these 
    revisions do not involve any physical changes to systems or 
    components, nor do they alter the typical manner in which the 
    systems or components are operated.
        No changes are being proposed to the type of testing currently 
    being performed, only to the length of the surveillance test 
    interval and to restrictions on conducting testing only during 
    shutdown conditions.
        Results of the review of historical 18 month surveillance data 
    and maintenance records support an increase in the surveillance test 
    intervals from 18 to 24 months (and up to 30 months on a non-routine 
    basis) because no potential for a significant increase in a failure 
    rate of a system or component was identified during these reviews.
        The proposed revision to reflect that the battery charger 
    performance test will continue to be conducted on a[n] 18 month 
    surveillance interval is an administrative change and does not alter 
    testing currently being performed.
        The proposed revision to the Bases to reflect that a change to a 
    24 month surveillance test interval is an exception to current 
    guidance is an administrative change and does not alter testing 
    currently being performed.
        3. Not involve a significant reduction in a margin of safety 
    because the results of the historical 18 month surveillance data and 
    maintenance records review identified no potential for a significant 
    increase in a failure rate of a system or component due to 
    increasing the surveillance test interval to 24 months. Existing 
    system and component redundancy is not being changed by these 
    proposed changes.
        There are no new or significant changes to the initial 
    conditions contributing to accident severity or consequences, 
    consequently there are no significant reductions in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: November 26, 1996
        Description of amendment request: The proposed changes would 
    eliminate the records retention requirements from the administrative 
    section of the Technical Specifications (TS) in accordance with NRC 
    Administrative Letter95-06, ``Relocation of Technical Specifications 
    Administrative Controls Related to Quality Assurance.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of the ... North Anna Power [Station] in 
    accordance with the proposed Technical Specifications changes will 
    not:
    
    [[Page 133]]
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The proposed 
    administrative changes do not affect equipment or its operation. 
    Therefore, the likelihood that an accident will occur is neither 
    increased nor decreased by relocating record retention requirements 
    from the Technical Specifications to the Operational Quality 
    Assurance Program. This TS change will not impact the function or 
    method of operation of plant equipment. Thus, a significant increase 
    in the probability of a previously analyzed accident does not result 
    due to this change. No systems, equipment, or components are 
    affected by the proposed changes. Thus, the consequences of any 
    accident previously evaluated in the UFSAR [Updated Final Safety 
    Analysis Report] are not increased by this change.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The proposed change 
    does not alter the design or operations of the physical plant. Since 
    record retention requirements are administrative in nature, a change 
    to these requirements does not contribute to accident initiation, an 
    administrative change related to this activity does not produce a 
    new accident scenario or produce a new type of equipment 
    malfunction. [These] changes do not alter any existing accident 
    scenarios. The proposed administrative change does not affect 
    equipment or its operation, and, thus, does not create the 
    possibility of a new or different kind of accident. Therefore, the 
    proposed change does not create the possibility of a new or 
    different kind of accident.
        (3) Involve a significant reduction in a margin of safety. 
    Section 6.0 of the North Anna ... Technical Specifications does not 
    have a basis description. The proposed administrative change does 
    not affect equipment or its operation, and, thus, does not involve 
    any reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Mark Reinhart, Acting
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: December 3, 1996
        Description of amendment request: This amendment request proposes 
    to revise the technical specifications associated with the inspection 
    of the reactor coolant flywheel to provide an exception to the 
    recommendations of Regulatory Guide 1.14, Revision 1, ``Reactor Coolant 
    Pump Flywheel Integrity.'' The proposed exception would allow either an 
    ultrasonic volumetric examination or surface examination to be 
    performed at approximately 10-year intervals. In addition, a correction 
    of the issuance date of a referenced regulatory guide is included.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is p presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The safety function of the RCP [reactor coolant pump] flywheels 
    is to provide a coastdown period during which the RCPs would 
    continue to provide reactor coolant flow to the reactor after loss 
    of power to the RCPs. The maximum loading on the RCP flywheel 
    results from overspeed following a LOCA [loss-of-coolant accident]. 
    The maximum obtainable speed in the event of a LOCA was predicted to 
    be less than 1500 rpm. Therefore, a peak LOCA speed of 1500 rpm is 
    used in the evaluation of RCP flywheel integrity in WCAP-14535. This 
    integrity evaluation shows a very high flaw tolerance for the 
    flywheels. The proposed change does not affect that evaluation. 
    Reduced coastdown times due to a single failed flywheel is bounded 
    by the locked rotor analysis, therefore, it would not place the 
    plant in an unanalyzed condition. Therefore, these changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment does not create the possibility of a new 
    or different kind of accident from any previously evaluated since 
    the proposed amendments will not change the physical plant or the 
    modes of plant operation defined in the facility operating license. 
    No new failure mode is introduced due to the proposed change, since 
    the proposed change does not involve the addition or modification of 
    equipment, nor do they alter the design or operation of affected 
    plant systems, structures, or components.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The operating limits and functional capabilities of the affected 
    systems, structures, and components are basically unchanged by the 
    proposed amendment. The results of the flywheel inspections 
    performed have identified no indications affecting flywheel 
    integrity. As identified in WCAP-14535, detailed stress analysis as 
    well as risk analysis have been completed with the results 
    indicating that there would be no change in the probability of 
    failure for RCP flywheels if all inspections were eliminated. 
    Therefore these changes do not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: December 3, 1996
        Description of amendment request: This amendment request proposes 
    to correct the reference to the Action Statement for Item 7.b, RWST 
    Level - Low-Low Coincident with Safety Injection, Table 3.3-3, 
    Engineered Safety Features Actuation System Instrumentation, from 
    Action 16 to Action 28.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Changing the reference from Action Statement 16 to Action 
    Statement 28 for Functional Unit 7.b. of Table 3.3-3 will reduce the 
    probability for an automatic switchover from the RWST [refueling 
    water storage tank] to an empty containment sump to occur, while an 
    RWST level channel is inoperable or is being tested with its 
    bistable tripped, should an inadvertent safety injection signal 
    occur concurrent with a single failure of a second RWST level 
    channel. The design of these channels does not allow for operation 
    or testing in bypass, so Action Statement 16 is not applicable. 
    Changing to Action Statement 28 will limit
    
    [[Page 134]]
    
    the duration that a channel could be inoperable or be in test with 
    its bistable bypassed. This change does not involve any design 
    changes or hardware modifications, and does not introduce any new 
    potential accident initiating conditions. The increase in allowed 
    outage time for this item was evaluated and the associated 
    unavailability and risk was shown to be equivalent to, or less than, 
    that of other functional units evaluated in WCAP-10271, Supplement 
    2, Revision 1. Therefore, this proposed change does not increase the 
    probability of any accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not result in any hardware changes and 
    does not result in a change in the manner in which the ESFAS 
    [engineered safety features actuation system] provides plant 
    protection. This change does not alter the functioning of the ESFAS. 
    Rather, the likelihood or probability of the ESFAS functioning 
    properly is affected as described above. This change will not change 
    the method by which any safety-related system performs its function. 
    Therefore, this proposed change will not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        This proposed change will not result in a significant reduction 
    in the margin of safety defined for any technical specification 
    since it does not alter the manner in which safety limits, limiting 
    safety system settings, or limiting conditions for operation are 
    determined.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: June 28, 1996
        Brief description of amendments: The amendment would modify the 
    technical specifications (TS) to increase the minimum required amount 
    of anhydrous trisodium phosphate (TSP) in the containment baskets. TSP 
    is used to ensure that following a postulated design basis loss of 
    coolant accident (LOCA), the containment sump pH is maintained greater 
    than or equal to seven.
        Date of issuance: December 10, 1996
        Effective date: December 10, 1996, to be implemented within 45 days 
    from the date of issuance.
        Amendment Nos.: Unit 1 - 110; Unit 2 - 102; Unit 3 - 82
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47962) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 10, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: June 21, 1996
        Brief description of amendments: The amendments revise the term 
    ``lifting loads'' used in Technical Specification 3.9.6b.2, Manipulator 
    Crane, to ``lifting force.'' This revision will clarify that the static 
    loads associated with the lifting tool, drive rod, and control rod 
    weights are not included in the lifting force limit.
        Date of issuance: December 12, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 171 and 153
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47977) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 12, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: February 22, 1996, and as 
    supplemented by letters dated July 4 and September 20, 1996
        Brief description of amendment: The amendment revises Clinton Power 
    Station Technical Specification 3.3.4.1, ``End of Cycle Recirculation 
    Pump Trip (EOC-RPT) Instrumentation,'' by deleting Surveillance 
    Requirement 3.3.4.1.6 which requires the RPT breaker interruption time 
    to be determined at least once per 60 months.
        Date of issuance: December 13, 1996
        Effective date: December 13, 1996
        Amendment No.: 111
    
    [[Page 135]]
    
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18169) The supplemental letters of July 4 and September 20, 1996, 
    provided clarifying information and did not include significant changes 
    relative to the original Federal Register notice.The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated December 13, 1996.No significant hazards consideration comments 
    received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of application for amendment: July 12, 1996, as 
    supplementedOctober 30, 1996.
        Brief description of amendment: The amendment revises TS 6.2.2.h 
    regarding the administrative controls for the normal working hours of 
    unit staff who perform safety-related functions, and TS 6.2.2.i 
    regarding an organizational change. The changes authorize (1) 
    establishment of unit staff work schedules that average 40 hours per 
    week using shifts as long as 12 hours, and (2) elimination of the 
    positions of General Supervisor Operations and Supervisor Operations.
        Date of issuance: December 12, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 158
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 14, 1996 (61 FR 
    42280) The October 30, 1996, letter provided supplemental information 
    that did not change the initial no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 12, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: July 12, 1996
        Brief description of amendment: The amendment revises Technical 
    Specification Section 6.2.2.i regarding the administrative controls for 
    the normal working hours of unit staff who perform safety-related 
    functions. The change allows the establishment of unit staff work 
    schedules that average 40 hours per week using shifts as long as 12 
    hours.
        Date of issuance: December 12, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 78
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 14, 1996 (61 FR 
    42281) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 12, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: July 28, 1995, as supplemented 
    October 25, 1995, and August 9, 1996
        Brief description of amendments: The amendments revise the 250 volt 
    DC profiles in the Technical Specifications for the two units to 
    reflect new load profile calculations.
        Date of issuance: December 17, 1996
        Effective date: Unit 1, as of date of issuance, to be implemented 
    within 30 days; Unit 2, as of date of issuance, to be implemented prior 
    to Startup following the Eighth Refueling and Inspection Outage for 
    Unit 2, which is scheduled for the Spring of 1997.
        Amendment Nos.: 162 and 133
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47622) The supplemental letters provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination nor the Federal Register notice.The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated December 17, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: June 12, 1992, as supplemented 
    September 17, 1992, March 17, 1993, August 17, 1993, August 18, 1993, 
    December 29, 1993, June 29, 1995, August 15, 1996, October 3, 
    1996,October 23, 1996, November 14, 1996, November 20, 1996 (JPN-96-
    045), November 20, 1996 (JPN-96-046), and November 27, 1996.
        Brief description of amendment: The amendment modifies
        Facility Operating License No. DPR-59 and the James A. FitzPatrick 
    Nuclear Power Plant (JAFNPP) Technical Specifications (TSs) to 
    authorize an increase in the maximum power level of JAFNPP from 2436 
    MWt to 2536 MWt. The amendment also approves changes to the TSs to 
    implement uprated power operation.
        Date of issuance: December 6, 1996
        Effective date:
        As of the date of issuance to be implemented upon plant startup 
    following the refueling outage cycle 13.
        Amendment No.: 239
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4943) The letters dated September 17, 1992, March 17, 1993, August 17, 
    1993, August 18, 1993, December 29, 1993, June 29, 1995, August 15, 
    1996,October 3, 1996, October 23, 1996, November 14, 1996, November 20, 
    1996, (JPN-96-045), November 20, 1996, (JPN-96-046), and November 27, 
    1996, provided clarifying information that did not change the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated December 6, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    [[Page 136]]
    
    Public Service Electric & Gas Company, Docket No. 50-311, Salem 
    Nuclear Generating Station, Unit No. 2, Salem County, New Jersey 
    Date of application for amendment: September 20, 1996, as 
    supplemented September 30, 1996
    
        Brief description of amendment: The amendment changes Technical 
    Specification Surveillance Requirement 4.7.7.b.4 for the Auxiliary 
    Building Exhaust Air Filtration System, and its associated Bases, to 
    indicate that the specified flowrate applies only to system testing.
        Date of issuance: December 12, 1996
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment No. 168
        Facility Operating License No. DPR-75: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55040) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 12, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: August 27, 1996, as 
    supplemented October 24, 1996
        Brief description of amendments: The amendment to Unit 2 deletes 
    License Condition 2.C.(24)(a) which required establishment by June 3, 
    1981, of regularly scheduled 8-hour shifts without reliance on routine 
    use of overtime. The amendments to both Units 1 and 2 revise Technical 
    Specification 6.2.2 to delete the reference to Generic Letter 82-12, 
    ``Nuclear Plant Staff Working Hours,'' and require that administrative 
    controls be established which will ensure that adequate shift coverage 
    is maintained without heavy use of overtime for individuals.
        Date of issuance: December 17, 1996
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos. 186 and 169
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications for both units and License for 
    Unit 2 only.
        Date of initial notice in Federal Register: September 12, 1996 (61 
    FR 48175) The October 24, 1996, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination or the original notice.The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated December 17, 1996.No significant hazards consideration 
    comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: May 29, 1996
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) Surveillance Requirement 3.5.1.4 to increase the 
    minimum boron concentration in the safety injections tanks from 1850 
    ppm to 2200 ppm.
        Date of issuance: December 6, 1996
        Effective date: December 6, 1996, to be implemented within 30 days 
    from the date of issuance.
        Amendment Nos.: Unit 2 - 135; Unit 3 - 124
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 31, 1996 (61 FR 
    40029) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 6, 1996. No significant 
    hazards consideration comments received: No.Temporary
        Local Public Document Room location: Science Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: September 27, 1996, as 
    supplemented on October 25, and November 18, 1996
        Brief description of amendment: The amendment revises Kewaunee 
    Nuclear Power Plant Technical Specification requirements related to the 
    low temperature overpressure protection (LTOP) system. Specifically, 
    the LTOP curve is modified to define 10 CFR Part 50, Appendix G 
    pressure temperature limitations for LTOP evaluation through the end of 
    operating cycle (EOC) 33. In addition, the LTOP enabling temperature 
    and the temperature required for starting a reactor coolant pump have 
    been changed consistent with the design basis for the LTOP system. 
    Finally, the TS bases were changed consistent with the changes 
    described above.
        Date of issuance: December 13, 1996
        Effective date: December 13, 1996, to be implemented within 30 
    days.
        Amendment No.: 130
        Facility Operating License No. DPR-43: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 7, 1996 (61 FR 
    52472) The October 25 and November 18, 1996, submittals provided 
    supplemental information that did not change the initial proposed no 
    significant hazards consideration determination.The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated December 13, 1996.No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
        Dated at Rockville, Maryland, this 24th day of December 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation
    [Doc. 96-33254 Filed 12-31-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
01/02/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X97-10102
Dates:
December 10, 1996, to be implemented within 45 days from the date of issuance.
Pages:
121-136 (16 pages)
PDF File:
x97-10102.pdf