X96-20131. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 21 (Wednesday, January 31, 1996)]
    [Notices]
    [Pages 3497-3508]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-20131]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from January 5, 1996, through January 19, 1996. 
    The last biweekly notice was published on January 22, 1996.
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By March 1, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above. 
    
    [[Page 3498]]
    
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: January 12, 1996
        Description of amendment request: Compliance with 10 CFR Part 50, 
    Appendix J, provides assurance that the primary containment, including 
    those systems and components that penetrate the primary containment, do 
    not exceed the allowable leakage rate values specified in the Technical 
    Specifications and Bases. The allowable leakage rate is determined so 
    that the leakage assumed in the safety analyses is not exceeded.
        On February 4, 1992, the NRC published a notice in the Federal 
    Register (57 FR 4166) discussing a planned initiative to begin 
    eliminating requirements marginal to safety that impose a significant 
    regulatory burden. Appendix J to 10 CFR Part 50, ``Primary Containment 
    Leakage Testing for Water-Cooled Power Reactors,'' was considered for 
    this initiative and the staff undertook a study of possible changes to 
    this regulation. The study examined the previous performance history of 
    domestic containments and examined the effect on risk of a revision to 
    the requirements of Appendix J. The results of this study are reported 
    in NUREG-1493, ``Performance-Based Leak-Test Program.''
        Based on the results of this study, the staff developed a 
    performance based approach to containment leakage rate testing. On 
    September 12, 1995, the NRC approved issuance of this revision to 10 
    CFR Part 50, Appendix J, which was subsequently published in the 
    Federal Register on September 26, 1995, and became effective on October 
    26, 1995. The revision added Option B ``Performance-Based 
    Requirements'' to Appendix J to allow licensees to voluntarily replace 
    the prescriptive testing requirements of Appendix J with testing 
    requirements based on both overall and individual component leakage 
    rate performance.
        Regulatory Guide 1.163, ``Performance-Based Containment Leak Test 
    Program,'' was developed as a method acceptable to the staff for 
    implementing Option B. Accordingly, the licensee has submitted, in its 
    application dated January 12, 1996, proposed changes to the TS to 
    implement 10 CFR Part 50, Appendix J, Option B, by referring to 
    Regulatory Guide 1.163, ``Performance-Based Containment Leakage-Test 
    Program.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1The proposed change will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Containment leak rate testing is not an initiator of any 
    accident; the proposed change does not affect reactor operations or 
    accident analysis, and has no significant radiological consequences. 
    Therefore, this proposed change will not involve an increase in the 
    probability or consequences of any previously-evaluated accident.
        2. The proposed change will not create the possibility of any 
    new accident not previously evaluated.
        The proposed change does not affect normal plant operations or 
    configuration, nor does it affect leak rate test methods. The test 
    history at Catawba (no ILRT [integrated leak rate test] failures) 
    provides continued assurance of the leak tightness of the 
    containment structure.
        3. There is no significant reduction in a margin of safety. 
        
    [[Page 3499]]
    
        The proposed changes are based on NRC-accepted provisions, and 
    maintain necessary levels of reliability of containment integrity. 
    The performanced-based approach to leakage rate testing recognizes 
    that historically good results of containment testing provide 
    appropriate assurance of future containment integrity; this supports 
    the conclusion that the impact on the health and safety of the 
    public as a result of extended test intervals is negligible.
        Based on the above, no significant hazards consideration is 
    created by the proposed change.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: December 27, 1995
        Description of amendment request: The proposed amendments would 
    modify Tables 3.3-11 and 4.3-7 of Beaver Valley Power Station Unit Nos. 
    1 and 2 (BVPS-1 and BVPS-2) Technical Specification (TS) 3.3.3.8 such 
    that only one valve position indication system for the power operated 
    relief valves and safety valves is required to be operable. The 
    licensee stated that the proposed amendments would then be consistent 
    with the NRC's Improved Standard Technical Specifications, NUREG-1431, 
    Revision 1, and with the guidance of Regulatory Guide 1.97, NUREG-0578, 
    and NUREG-0737.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change involves instrumentation which is redundant 
    in monitoring the position of valves and, as such, does not 
    influence the potential for an initiating event involving the power 
    operated relief valves (PORVs) or the safety valves (SVs). 
    Implementation of these changes will reduce the potential for 
    challenges to the plant due to a potential shutdown which should not 
    be necessary due to the restrictive nature of having unnecessary 
    redundant position indication in the technical specification. By 
    deleting the Unit No. 1 technical specification operability 
    requirements for the PORV acoustic detectors, and by deleting, on 
    both units, the technical specification operability requirements for 
    the SV temperature detector position indicators, the potential for 
    unnecessary shutdowns is reduced. When inoperable, the PORV acoustic 
    detectors and the SV temperature detectors presently invoke an 
    unnecessary action statement as another fully qualified safety-
    related position indication system exists to provide indication. The 
    proposed change modifies Specification 3.3.3.8 actions and 
    surveillance requirements, but does not affect the BASES.
        The remaining instrumentation on these tables [3.3-11 and 4.3-7] 
    will be unaffected. The remaining position indication systems for 
    the PORVs and SVs are fully qualified and satisfy regulatory 
    criteria for post accident monitoring of valve position. These 
    changes do not affect the ability to satisfy analysis assumptions 
    regarding operation of the PORVs and SVs. They do not affect the 
    ability to continue to meet the guidance of Regulatory Guide 1.97, 
    the post Three Mile Island criteria contained in NUREG 0578 and 
    NUREG 0737, and reflect the guidance provided in NUREG 1431, 
    ``Improved Standard Technical Specifications'' (ISTS). Therefore, we 
    have concluded that these changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated in the Updated Final Safety Analysis Report 
    (UFSAR).
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change will reduce the potential to challenge 
    safety systems due to eliminating the potential for unnecessary 
    plant shutdowns. The proposed changes are limited to PORV and SV 
    position indication and do not involve any physical changes to the 
    PORVs or SVs or their setpoints. These changes do not delete any 
    design basis accident functions previously provided by the PORVs or 
    SVs nor has the probability of inadvertent opening been increased. 
    Accordingly, no new single failure has been identified as a result 
    of these changes. Therefore, these changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated in the UFSAR.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes have been incorporated to eliminate a 
    degree of equipment redundancy and is consistent with the Improved 
    Standard Technical Specifications (ISTS). The Unit No. 1 
    specification presently requires operability of both redundant PORV 
    position indication systems and the primary and backup SV position 
    indication systems. The Unit No. 2 specification also requires 
    operability of the primary and backup SV position indication 
    systems. These changes will potentially eliminate some challenges 
    and potential unnecessary shutdowns by eliminating equipment 
    determined to be no longer necessary. Only one safety-related 
    position indication system is necessary to satisfy regulatory 
    criteria; therefore, operation of the plant in accordance with the 
    proposed amendment would not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of amendment request: December 22, 1995
        Description of amendment request: The proposed amendment would 
    revise the Duane Arnold Energy Center (DAEC) Technical Specifications 
    (TS) Sections 3.7.A and 4.7.A, ``Primary Containment,'' by deleting 
    information also contained in 10 CFR Part 50, Appendix J, Option A and 
    incorporating references to the Primary Containment Leakage Rate 
    Testing Program. These changes will allow the use of the performance 
    based option of containment leak testing. The request also adds 
    Operability and Surveillance Requirements (SRs) for the drywell air 
    lock. Minor administrative changes are also made. These changes are 
    consistent with comparable specifications in the Improved Standard 
    Technical Specifications (ITS), NUREG-1433. In addition to the 
    licensee's proposed revision to the DAEC TS, the staff will be 
    executing administrative changes and corrections to the TS Bases, as 
    submitted in letters(2) dated February 13, 1995. Sections that will be 
    changed or corrected are Section 1.2, Bases; Section 2.2, Bases Reactor 
    Coolant System Integrity; Section 3.2, Bases; Section 3.7.H/4.7.H, 
    Bases Containment Atmosphere Dilution; and Section 3.7.I/4.7.I, Bases 
    Oxygen Concentration.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    
    [[Page 3500]]
    consideration, which is presented below:
        . The proposed revision does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Information contained in 10 CFR 50, Appendix J was deleted and 
    references to the Primary Containment Leakage Rate Testing Program 
    were added. These are administrative changes to allow the use of 
    performance-based containment leakage testing methods. The 
    containment testing program will conform with the requirements of 
    Option B of 10 CFR Part 50, Appendix J and approved exemptions. The 
    performance of the leakage tests themselves is not an input or 
    consideration in any accident previously evaluated, thus the 
    proposed change will not increase the probability of any such 
    accident occurring. The same operability requirements remain for the 
    primary containment, therefore the consequences of an accident are 
    not significantly increased.
        Drywell air lock operability and surveillance requirements were 
    added. Actions for one air lock door inoperable have been added 
    consistent with the ITS. In addition, notes have been added to allow 
    entry and exit to perform repairs of the air lock components and to 
    explain that the previous overall leak test is not invalidated by an 
    inoperable door. This change represents an additional restriction on 
    plant operation, since the previous condition of one air lock door 
    inoperable did not require any actions to be taken. A requirement to 
    verify proper operation of interlock mechanism was also added. This 
    will ensure that one door is always closed which maintains primary 
    containment integrity.
        The addition of these new drywell air lock requirements provides 
    more stringent provisions than previously existed in the [current 
    Technical Specifications]. The more stringent requirements will not 
    result in operation that will increase the probability of initiating 
    an analyzed event. If anything, the new requirements may decrease 
    the probability or consequences of an analyzed event by 
    incorporating the more restrictive changes discussed above. These 
    changes will not alter assumptions relative to mitigation of an 
    accident or transient event. The more restrictive requirements will 
    not alter the operation of process variables, structures, systems, 
    or components as described in the safety analyses.
        The TS revision includes the relocation of certain requirements 
    from the current technical specification (CTS) to licensee 
    controlled documents. CTS 4.7.A.1.e contains a requirement to 
    replace the T-ring inflatable seals for the 18 inch purge valves 
    every four years. This provision is not in the ITS as it is a 
    maintenance issue and not a surveillance for operability. CTS 
    4.7.A.1.e also contains a requirement to verify (during Type C 
    testing) that the mechanical modification which limits the maximum 
    opening angle for the 18 inch purge valves is intact. The ITS only 
    requires this surveillance if the mechanical modification is not 
    permanent. At DAEC, the 18 inch purge valves are permanently blocked 
    to restrict opening to 30 deg.. These CTS provisions will be 
    relocated to plant procedures. Any changes to these relocated 
    requirements will require an evaluation in accordance with 10 CFR 
    50.59. CTS 4.7.A.1.a and 4.7.A.1.d contain some procedural details 
    that are not contained in Appendix J. These details will also be 
    relocated to plant procedures, consistent with the ITS. Since any 
    changes to these licensee controlled documents will be evaluated in 
    accordance with 10 CFR 50.59, no significant increase in the 
    probability or consequences of an accident previously evaluated will 
    be allowed.
        The proposed revision does not involve any change to the 
    configuration or method of operation of any plant equipment that is 
    used to mitigate the consequences of an accident, nor does it affect 
    any assumptions or conditions in the accident analysis. The proposed 
    revision does not degrade any existing plant programs, nor modify 
    any functions of safety related systems or accident mitigation 
    functions previously credited at the DAEC. The proposed changes do 
    not impact initiators of analyzed events. They also do not impact 
    the assumed mitigation of accidents or transient events. These TS 
    changes will not alter assumptions made in the safety analysis and 
    licensing basis.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed revision does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Deleting information from the TS which is contained in 10 CFR 
    50, Appendix J and adding references to the Primary Containment 
    Leakage Rate Testing Program are purely administrative changes to 
    allow the use of performance-based containment leakage testing 
    methods. The containment testing program will conform with the 
    requirements of Option B of 10 CFR Part 50, Appendix J and approved 
    exemptions. The use of Option B will maintain the containment safety 
    functions as a barrier to the release of radioactivity to the 
    environment.
        The proposed revision does not make any physical or operational 
    changes to existing plant systems or components, nor does it alter 
    any plant parameters, revise any safety limit setpoint, or provide 
    any new release pathways. The proposed revision does not change any 
    transient responses assumed in the Design Bases of the plant.
        The proposed changes which relocate requirements to licensee 
    controlled documents will not alter the plant configuration (no new 
    or different type of equipment will be installed) or change the 
    methods governing normal plant operation. These changes will not 
    alter assumptions made in the safety analysis or licensing basis.
        The proposed changes which add more restrictive requirements to 
    the CTS will not alter the plant configuration (no new or different 
    type of equipment will be installed) or change the methods governing 
    normal plant operation. These changes do impose different 
    requirements. However, they are consistent with assumptions made in 
    the safety analyses.
        Therefore, the revision does not create the possibility of a new 
    or different kind of accident previously evaluated.
        3. The proposed revision will not significantly reduce any margin 
    of safety.
        Deleting information from the TS which is contained in 10 CFR 
    50, Appendix J and adding references to the Primary Containment 
    Leakage Rate Testing Program do not involve a significant reduction 
    in the margin of safety. These changes are administrative in nature 
    and either eliminate a redundant requirement or clarify the 
    applicability and acceptability of an alternative, NRC approved, 
    leak rate testing provision within the TS. The containment testing 
    program will conform to the requirements of Option B of 10 CFR Part 
    50, Appendix J and approved exemptions. The use of Option B will 
    maintain the containment safety functions as a barrier to the 
    release of radioactivity to the environment.
        The proposed revision does not require any modifications to 
    existing plant systems or equipment, safety limit settings, or 
    parameters utilized in the licensing bases for the safety analysis. 
    The proposed revision does not change any safety analysis or any 
    accident mitigation action for which DAEC has previously taken 
    credit. The proposed changes do not involve any technical changes; 
    they have no impact on any safety analysis assumptions. The addition 
    of new requirements either increases or does not affect the margin 
    of safety.
        The proposed changes that relocate requirements from the CTS to 
    licensee controlled documents will not reduce a margin of safety 
    since they have no impact on any safety analysis assumptions. In 
    addition, the requirements to be relocated from the CTS to the 
    licensee controlled document are unchanged. Since any future changes 
    to this licensee controlled document will be evaluated in accordance 
    with the requirements of 10 CFR 50.59, no significant reduction in a 
    margin of safety will be allowed.
        The proposed changes are consistent with NUREG-1433, which was 
    approved by the NRC Staff. The changes are also consistent with NRC 
    guidance provided for the implementation of Option B. The change 
    controls for proposed relocated details and requirements are 
    acceptable. Therefore, revising the TS to reflect the NRC accepted 
    level of detail and requirements ensures that there is no reduction 
    in a margin of safety.
        Therefore, the proposed revision will not significantly reduce 
    any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401 
    
    [[Page 3501]]
    
        Attorney for licensee: Jack Newman, Kathleen H. Shea, Morgan, 
    Lewis, & Bockius, 1800 M Street, NW., Washington, DC 20036-5869
        NRC Project Director: Gail H. Marcus
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of amendment request: December 14, 1995
        Description of amendment request: The proposed amendment would 
    modify Technical Specifications 3.3.1.1, ``Reactor Protection System 
    (RPS) Instrumentation,'' and 3.3.6.1, ``Primary Containment and Drywell 
    Isolation Instrumentation,'' to eliminate periodic response time 
    testing of selected analog trip modules (ATMs). This request is 
    supported by analyses prepared by the Boiling Water Reactor Owners' 
    Group topical report NEDO-32291, ``System Analyses for Elimination of 
    Selected Response Time Testing Requirements,'' which demonstrate that 
    other periodic tests required by technical specifications, such as 
    channel calibrations, channel functional tests and logic system 
    functional tests, are adequate to ensure ATM response times remain 
    within acceptable limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        (1) The purpose of the proposed Technical Specification (TS) 
    change is to eliminate response time testing requirements for 
    selected analog trip modules (ATMs) in the Reactor Protection System 
    (RPS) and the main steam isolation valve (MSIV) isolation actuation 
    instrumentation. The Boiling Water Reactor Owners' Group (BWROG) has 
    completed an evaluation which demonstrates that response time 
    testing is redundant to the other TS-required testing. These other 
    tests, in conjunction with actions taken in response to NRC Bulletin 
    90-01, ``Loss of Fill-Oil in Transmitters Manufactured by 
    Rosemount,'' and Supplement 1, are sufficient to identify failure 
    modes or degradations in instrument response time and ensure 
    operation of the associated systems within acceptable limits. There 
    are no known failure modes that can be detected by response time 
    testing that cannot also be detected by other TS-required testing. 
    This evaluation was documented in NEDO-32291, ``System Analyses for 
    Elimination of Selected Response Time Testing Requirements,'' 
    January 1994. Illinois Power (IP) has confirmed the applicability of 
    this evaluation to Clinton Power Station (CPS). In addition, IP has 
    completed the actions identified in the NRC staff's safety 
    evaluation of NEDO-32291.
        Because of the continued application of other existing TS-
    required tests such as channel calibrations, channel checks, channel 
    functional tests, and logic system functional tests, the response 
    time of these systems will be maintained within the acceptance 
    limits assumed in plant safety analyses and required for successful 
    mitigation of an initiating event. The proposed changes do not 
    affect the capability of the associated systems to perform their 
    intended function within their required response time, nor do the 
    proposed changes themselves affect the operation of any equipment. 
    As a result, IP has concluded that the proposed changes do not 
    involve a significant increase in the probability or the 
    consequences of an accident previously evaluated.
        (2) The proposed changes only apply to the testing requirements 
    for ATMs in the systems identified above and do not result in any 
    physical change to these or other components or their operation. As 
    a result, no new failure modes are introduced. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        (3) The current TS-required response times are based on the 
    maximum values assumed in the plant safety analyses. These analyses 
    conservatively establish the margin of safety. As described above, 
    the proposed changes do not affect the capability of the associated 
    systems to perform their intended function within the allowed 
    response time used as the basis for the plant safety analyses. The 
    potential failure modes for the components within the scope of this 
    request were evaluated for impact on instrument response time. This 
    evaluation confirmed that the remaining TS-required testing is 
    sufficient to identify failure modes or degradations in instrument 
    response times and to ensure that operation of the instrumentation 
    within the scope of this request is within acceptable limits. As a 
    result, it has been concluded that plant and system response to an 
    initiating event will remain in compliance with the assumptions of 
    the safety analysis.
        Further, although not explicitly evaluated, the proposed changes 
    will provide an improvement to plant safety and operation by 
    reducing the time safety systems are unavailable, reducing the 
    potential for safety system actuations, reducing plant shutdown 
    risk, limiting radiation exposure to plant personnel, and 
    eliminating the diversion of key personnel resources to conduct 
    unnecessary testing. Therefore, IP has concluded that this request 
    will result in an overall increase in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
        Attorney for licensee: Sheldon Zabel, Esq., Schiff, Hardin and 
    Waite, 7200 Sears Tower, 233 Wacker Drive, Chicago, Illinois 60606
        NRC Project Director: Gail H. Marcus
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: December 11, 1995
        Description of amendment request: The proposed amendment would 
    modify Technical Specification (TS) Section 4.7, Surveillance 
    Requirements for Primary Containment Automatic Isolation Valves. 
    Specifically, the proposed amendment would delete TS Surveillance 
    Requirement 4.7.D.4, which requires replacement of the seat seals for 
    the drywell and suppression chamber purge and vent valves every 5 
    years.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        An evaluation of the operational performance of the 18-inch 
    purge and vent valves has concluded that deletion of the Monticello 
    Technical Specification surveillance requirement 4.7.D.4 will have 
    no adverse impact on the seat leakage performance of these primary 
    containment isolation valves, no adverse impact on the testing 
    performed in accordance with 10 CFR 50, Appendix J, and thus no 
    adverse impact on the containment isolation function of these 
    primary containment isolation valves. The material of which the T-
    shaped elastomer seat is comprised of has been found to withstand 
    normal and accident thermal exposures for the design life of the 
    plant based on a thermal aging analysis. Radiation effects will not 
    have an adverse impact on the elastomer seat material. Therefore, 
    this amendment will not cause a significant increase in the 
    probability or consequences of an accident previously evaluated for 
    the Monticello plant.
        The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The proposed change to the Technical Specifications for the 
    Primary Containment Purge and Vent valves does not alter the 
    function of these components or their interrelationships with other 
    systems. Therefore, this amendment will not create the possibility 
    of a new or different kind of accident from any accident previously 
    analyzed.
        The proposed amendment will not involve a significant reduction 
    in the margin of safety.
        The operating experience of these valves has demonstrated that 
    the testing performed 
    
    [[Page 3502]]
    in accordance with 10 CFR 50, Appendix J, provides a high level of 
    confidence in the ability of these valves to perform their safety 
    function with respect to valve leak tightness. The proposed 
    amendment will not involve a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: December 27, 1995
        Description of amendment requests: The amendments would revise the 
    combined Technical Specifications (TS) 3/4.6.1.1, ``Containment 
    Integrity;'' 3/4.6.1.2, ``Containment Leakage;'' 3/4.6.1.3, 
    ``Containment Air Locks;'' 3/4.6.1.6, ``Containment Structural 
    Integrity;'' 3/4.6.3, ``Containment Isolation Valves;'' and their 
    associated Bases; and would add TS 6.8.4.j, ``Containment Leakage Rate 
    Testing Program,'' to implement the performance-based leakage rate 
    testing program, as permitted by 10 CFR Part 50, Appendix J. These 
    changes will support the implementation of the performance-based 
    testing of Option B to Appendix J for Types A, B, and C containment 
    leakage rate testing and the appropriate rescheduling of testing. The 
    amendment changes the TS to implement 10 CFR Part 50, Appendix J, 
    Option B, by referring to Regulatory Guide 1.163, ``Performance-Based 
    Containment Leakage Test Program.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes to Technical Specification (TS) 3/4.6.1.1, 
    3/4.6.1.2, 3/4.6.1.3, 3/4.6.1.6, 3/4.6.3, and the addition of 6.8.4 
    j., to implement the performance-based Containment Leakage Rate 
    Testing Program have no effect on plant operation. The proposed 
    changes only provide mechanisms within the TS for implementing a 
    performance-based methodology for determining the frequency of leak 
    rate testing that has been approved by the Commission. The test type 
    and test method used for testing would not be changed. The test 
    acceptance criteria would not be changed, and containment leakage 
    will continue to be maintained within the required limits.
        Directly referencing the Containment Leakage Rate Testing 
    Program for containment ILRT [integrated leak rate testing] and LLRT 
    [local leak rate test] requirements does not involve any 
    modification to plant equipment or affect the operation or design 
    basis of the containment. Leakage rate testing is not a precursor to 
    or an initiating event for any accident.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes only allow for the implementation of 10 CFR 
    50, Appendix J, Option B, testing frequencies and do not involve any 
    modifications to any plant equipment or affect the operation or 
    design basis of the containment. The proposed changes do not affect 
    the response of the containment during a design basis accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect or change a Safety Limit or 
    affect plant operations. The changes only implement the allowed 10 
    CFR 50, Appendix J, Option B testing frequencies that have been 
    determined by the Commission not to involve a safety concern. The 
    testing method, acceptance criteria, and basis for testing are not 
    changed and still provide assurance that the containment will 
    provide its intended function.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Saxton Nuclear Experimental Corporation (SNEC), Docket No. 50-146, 
    Saxton Nuclear Experimental Facility (SNEF), Bedford County, 
    Pennsylvania
    
        Date of amendment request: November 21, 1995.
        Description of amendment request: The proposed amendment would 
    change the license and technical specifications to add GPU Nuclear 
    Corporation (GPUN) as a licensee for the SNEF along with SNEC and would 
    transfer from SNEC to GPUN all management-related responsibilities for 
    the SNEF. Responsibility for safely maintaining the containment vessel 
    and performing characterization activities would change from SNEC to 
    GPUN. Technical specification organizational positions would be changed 
    from SNEC titles to GPUN titles. GPUN would take responsibility from 
    SNEC for administration of all SNEF functions, for radiation safety 
    activities, and for providing on-site management and continuing 
    oversight of production activities. The appointment of members to the 
    Saxton Radiation Safety Committee and the reporting of the Committee 
    would change from the SNEC President to the GPUN Vice President of the 
    Nuclear Services Division. The GPUN President would have the authority 
    to request audits and would receive audit reports instead of the SNEC 
    President. Procedure control methodology and the administrative 
    procedure for procedures would be changed from SNEC procedures to GPUN 
    procedures. The responsibility for records retention and reporting 
    would change from SNEC to GPUN. The organization chart for the facility 
    would be changed to reflect the addition of GPUN as a licensee.
        Basis for proposed no significant Hazards Consideration 
    Determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve a significant hazards 
    considerations because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Because the proposed changes are administrative in nature they 
    would have no effect on the likelihood or impact on the potential 
    accidents of fire, flood or radiological hazard. 
    
    [[Page 3503]]
    
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        Because the proposed changes are administrative in nature they 
    would not create the possibility of a new or different kind of 
    accident from any accident previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        Because the proposed changes are administrative in nature they 
    would not involve any reduction in a margin of safety.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678 Attorney for the Licensee: 
    Ernest L. Blake, Jr., Esquire, Shaw, Pittman, Potts, and Trowbridge, 
    2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Seymour H. Weiss
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: January 4, 1996 (TS 95-22)
        Description of amendment request: The proposed change would extend 
    the functional testing interval for the following isolation radiation 
    monitor instruments from monthly to quarterly: (1) Engineered Safety 
    Feature Actuation System Instrumentation Surveillance Requirements 
    Table 4.3-2, Item 3.c.3, Containment Purge Air Exhaust Monitor 
    Radioactivity-High; (2) Radiation Monitoring Instrumentation 
    Surveillance Requirements Table 4.3-3, Item 1.a, Fuel Storage Pool Area 
    Radiation Monitor; (3) Table 4.3-3, Item 2.a, Containment Purge Air 
    Exhaust; (4) Table 4.3-3, Item 2.b.i, Containment Gaseous Activity RCS 
    Leakage Detection; (5) Table 4.3-3, Item 2.b.ii, Containment 
    Particulate Activity RCS Leakage Detection; and (6) Table 4.3-3, Item 
    2.c, Control Room Isolation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Review of the past history for the affected and similar 
    radiation monitors revealed that extending the functional testing 
    interval for these monitors will not adversely affect system 
    operability and will effectively increase system availability. These 
    radiation monitors are not accident initiating equipment, thus 
    increasing the surveillance interval on these monitors will not 
    affect the probability of any accident previously evaluated. Based 
    on the above statements, it is concluded that the probability or 
    consequences of an accident previously evaluated is not increased.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        No new type of accident or malfunction will be created since the 
    radiation monitors are not accident initiating equipment. The 
    proposed change merely increases the functional testing interval for 
    the affected radiation monitors, and does not change the method and 
    manner of plant operation. The safety design bases in the Updated 
    Final Safety Analysis Report have not been altered.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes do not change the plant configuration in a 
    way that introduces a new potential hazard to the plant and do not 
    involve a significant reduction in the margin of safety. The 
    proposed changes do not affect applicable safety analysis acceptance 
    criteria and will not affect system operating conditions. 
    Additionally, plant operating experience with similar monitors has 
    shown that there has not been additional failures due to the 
    quarterly testing frequency. Thus, it is concluded that the margin 
    of safety is not reduced.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: November 22, 1995
        Description of amendment request: The proposed amendment replaces 
    the requirements associated with the boron dilution mitigation system 
    (BDMS) in the Wolf Creek Generating Station Technical Specifications 
    with alarms, indicators, procedures, and controls to assure proper 
    resolution of potential inadvertent boron dilution events.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        . The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The only event potentially impacted by the proposed change is 
    the inadvertent boron dilution event. The discussion of the 
    probability and consequences of an inadvertent boron dilution event 
    at WCGS is provided in USAR [Updated Safety Analysis Report] Section 
    15.4.6. Primarily, the proposed changes revise the method of 
    detecting and mitigating the event. The only aspect of the changes 
    that impact[s] the potential causes of an inadvertent boron dilution 
    event is the increased requirement to isolate potential dilution 
    sources in Modes 3, 4 and 5. As a result, the overall probability of 
    the event is slightly decreased.
        The alternate methods to detect and mitigate this event achieve 
    the same basic goal as the current BDMS; to prevent a return to 
    critical during an inadvertent dilution event. The proposed changes 
    to the BDMS will result in an improved system that will provide an 
    improved response to the inadvertent boron dilution event, and that 
    will prevent a return to critical. Thus, it can be concluded that 
    the proposed change will not significantly increase the consequences 
    of a postulated inadvertent boron dilution event.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The revisions to plant procedural requirements to either operate 
    a reactor coolant pump or to isolate/control potential dilution 
    sources does [sic] not create the potential for a new or different 
    kind of accident because these new requirements are configurations 
    which have always been allowed. Similarly, the new normal position 
    for the letdown divert valve does not create a new or different 
    accident because the new normal position has always been an allowed 
    position. The other procedural changes only increase the plant 
    operators' awareness of potential boron dilution problems or provide 
    the steps needed to respond to available indications and alarms to 
    mitigate the potential event. As a result, these procedural changes 
    do not create the possibility of a new or different kind of 
    accident.
        The proposed changes also include addition of new redundant VCT 
    high level alarms and a new alarm indicating that the 
    
    [[Page 3504]]
    letdown divert valve is not in the ``VCT'' position. Because the alarms 
    are passive, they do not create the possibility of a new or 
    different kind of accident.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The design criterion and margin of safety for the current BDMS 
    is that the dilution event is terminated prior to the loss of all 
    shutdown margin. The same criterion will be met following the 
    implementation of the proposed changes. Therefore, there is no 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: December 20, 1995
        Description of amendment request: This amendment request proposes 
    to revise Technical Specification 3/4.6.1.1, ``Containment Integrity,'' 
    and 3/4.6.1.3, ``Containment Air Locks,'' and to add Technical 
    Specification 6.8.4i, ``Containment Leakage Rate Testing Program,'' to 
    implement the new performance-based leakage rate testing program as 
    permitted by 10 CFR 50, Appendix J. Also, Technical Specification 1.7e, 
    ``Containment Integrity,'' would be revised to reference Technical 
    Specification 4.6.1.1.c. These proposed changes will implement the 
    performance-based testing of Option B to Appendix J, for Type A, B, and 
    C containment leak testing by referring to Regulatory Guide 1.163, 
    ``Performance-Based Containment Leakage-Test Program.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes to Technical Specifications 3/4.6.1.1 and 
    3/4.6.1.3, and the addition of Technical Specification 6.8.4i to 
    implement the new performance based Containment Leakage Rate Testing 
    Program, have no effect on plant operation. The proposed changes 
    only provide mechanisms within the technical specifications for 
    implementing a performance-based methodology, for determining the 
    frequency of leak rate testing, which has been approved by the NRC. 
    The test type and test method used for testing would not be changed. 
    The test acceptance criteria would not be changed, and containment 
    leakage will continue to be maintained within the required limits.
        Directly referencing the Containment Leakage Rate Testing 
    Program for containment integrated leak rate test and local leak 
    rate test requirements does not involve any modification to plant 
    equipment or affect the operation or design basis of the 
    containment. Leakage rate testing is not a precursor to or an 
    initiating event for any accident.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes only allow for implementation of 10 CFR 50, 
    Appendix J, Option B, testing frequencies and do not involve any 
    modifications to any plant equipment or affect the operation or 
    design basis of the containment. The proposed changes do not affect 
    the response of the containment during a design basis accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect or change a Safety Limit, any 
    limiting condition for operation or affect plant operations. The 
    changes only implement the allowed Option B testing frequencies that 
    have been determined by the NRC not to involve a safety concern. The 
    testing method, acceptance criteria, and bases are not changed and 
    still provide assurance that the containment will provide its 
    intended function.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved. 
    
    [[Page 3505]]
    
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: November 14, 1995, as 
    supplemented January 4, 1996.
        Brief description of amendments: The amendments revise the 
    Technical Specifications to incorporate 10 CFR Part 50, Appendix J, 
    ``Primary Reactor Containment Leakage Testing for Water-Cooled Power 
    Reactors,'' Option B. Technical Specification changes for the LaSalle 
    facility will be addressed under separate correspondence.
        Date of issuance: January 11, 1996
        Effective date: January 11, 1996
        Amendment Nos.: 148, 142, 169, and 165
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1995 (60 FR 
    62896). The January 4, 1996, supplement provided a specific 
    implementation date for the requested amenement. This information was 
    within the scope of the original application and did not change the 
    staff's initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 11, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of application for amendment: November 14, 1995
        Brief description of amendment: The amendment revises the Haddam 
    Neck Technical Specifications (TS) to provide an one-time exception to 
    TS 3.9.12, '' Fuel Building Storage Air Cleanup System,'' to allow the 
    fuel storage building air cleanup system to be inoperable for a limited 
    duration during intervals in which new fuel rack modules will be moved 
    into and old fuel rack modules will be moved out of the fuel storage 
    building.
        Date of Issuance: January 17, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 187
        Facility Operating License No. DPR-61. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 28, 1995 (60 
    FR 58688) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated January 17, 1996 No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan Date of application for amendment: 
    November 8, 1995, as supplemented November 17, 1995
    
        Brief description of amendment: The amendment removes the 
    prescriptive Type A containment leakage test rate frequency of 40 plus 
    or minus 10 months and adds a reference to perform containment leakage 
    rate tests in accordance with the criteria specified in Appendix J of 
    10 CFR Part 50 as modified by approved exemptions. In addition, the 
    amendment revises the test pressure for Type B and C testing to correct 
    a typographical error.
        Date of issuance: January 16, 1996
        Effective date: January 16, 1996
        Amendment No.: 117
        Facility Operating License No. DPR-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62489) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated January 16, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: March 29, 1995, as supplemented 
    by letters dated September 18 and November 16, 1995
        Brief description of amendments: The amendments revise Technical 
    Specification requirements for the Low Temperature Overpressure 
    Protection system and update the heatup and cooldown curves for both 
    units.
        Date of issuance: January 11, 1996
        Effective date: As of the date of issuance to be implemented within 
    60 days
        Amendment Nos.:  Unit 1 - 162; Unit 2 - 144
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications. Date of initial notice in Federal 
    Register: September 27, 1995 (60 FR 49933) The September 18 and 
    November 16, 1995, letters provided clarifying information that did not 
    change the scope of the March 29, 1995, application and the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated January 11, 1996. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of application for amendments: December 2, 1994
        Brief description of amendments: The amendments replace Appendix B, 
    ``Environmental Technical Specifications,'' with an Environmental 
    Protection Plan (Nonradiological) and revise the Operating Licenses to 
    reflect these changes.
        Date of issuance: December 19, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: Unit 1 - 199 - Unit 2 - 140
        Facility Operating License Nos. DPR-57 and NPF-5. Amendments 
    revised the Technical Specifications and Operating Licenses.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    502) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 19, 1995. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513 
    
    [[Page 3506]]
    
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: March 17, 1995, as supplemented 
    by letter dated July 6, 1995
        Brief description of amendments: The amendments revise Technical 
    Specification 3/4.9.4, Containment Building Penetrations, to allow the 
    personnel airlock to be open during core alterations or movement of 
    irradiated fuel within the containment.
        Date of issuance: November 30, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 92 and 70
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35077) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 30, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: August 17, 1995, as supplemented by 
    letters dated November 22, and December 18, 20, and 27, 1995
        Brief description of amendment: The amendment revised the primary 
    containment air lock technical specifications to allow the air locks to 
    be open in Mode 5 (refueling) during core alterations except for 
    movement of recently irradiated fuel. All other provisions of the 
    August 17, 1995, requests are defered.
        Date of issuance: January 11, 1996
        Effective date: January 11, 1996
        Amendment No.: 85
        Facility Operating License No. NPF-47. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47619) The additional information contained in the supplemental 
    letters dated November 22, and December 18, 20, and 27, 1995, was 
    clarifying in nature and thus, within the scope of the initial notice 
    and did not affect the staff's proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated Janaury 11, 1996. 
    No significant hazards consideration comments received. No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 20, 1995
        Brief description of amendment: The proposed amendment revised the 
    technical specifications to eliminate the response time testing 
    requirements for selected Reactor Protection System Instrumentation.
        Date of issuance: January 11, 1996
        Effective date: January 11, 1996
        Amendment No.: 86
        Facility Operating License No. NPF-47. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62492) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated Janaury 11, 1996. No significant 
    hazards consideration comments received. No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: May 25, 1995 (AEP:NRC:1071T)
        Brief description of amendments: The amendments incorporate a 
    cycle- and burnup-dependent peaking factor penalty in the Core 
    Operating Limits Report and add an appropriate reference to the COLR 
    and update the topical report reference in the Technical 
    Specifications.
        Date of issuance: January 4, 1996
        Effective date: January 4, 1996, with full implementation within 45 
    days
        Amendment Nos.: Unit 1, 206, Unit 2, 190
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register:  The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated January 4, 1996. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: October 3, 1995
        Brief description of amendment: The amendment removes the Limiting 
    Condition for Operation (LCO) and Surveillance Requirements for the 
    loss-of-normal power (LNP) trip function from Tables 3.2.2 and 4.2.1 
    and inserts new LCO 3.2.F and Surveillance Requirement 4.2.F. In 
    addition, the amendment adds a new table to specify the required LNP 
    instrumentation for each bus, updates the Table of Contents, makes some 
    editorial changes, and revises the associated Bases section.
        Date of issuance: January 17, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 92
        Facility Operating License No. DPR-21. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1995 (60 FR 
    62111) The Commission's related evaluation of the amendment is 
    contained in a Safety evaluation dated January 17, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: September 11, 1995, as 
    supplemented November 15, 1995.
        Brief description of amendment: The amendment changes Technical 
    Specification Sections 3.4.8 and 3.9.9, Tables 2.2-1, 3.3-3, 3.3-5 and 
    3.3-8, and Bases Sections 3/4.2.1, 3/4.4.8 and 3/4.11.2.1. These 
    changes combine several different administrative changes which will 
    correct typographical errors, provide clarifications, or make editorial 
    changes.
        Date of issuance: January 17, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 194 
        
    [[Page 3507]]
    
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52933) The November 15, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated January 17, 1996. 
    No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: September 29, 1995, as 
    supplemented November 9, 1995.
        Brief description of amendment: The amendment provides three 
    changes to the Technical Specifications (TS) relating to the 
    pressurizer safety valves (PSV) and the main steam safety valves 
    (MSSV).
        The first change is to TS 3.4.2.1 and 3.4.2.2 and involves relaxing 
    the as-found setpoint tolerance for the pressurizer safety valves 
    (PSVs) and the main steam safety valves (MSSVs) from the current value 
    of plus or minus 1% to plus or minus 3%. Table 4.7-1 is also modified 
    to correct the as-found tolerance for the MSSV from plus or minus 1% to 
    plus or minus 3%. Notes are added to TS 3.4.2.2 and Table 4.7-1 which 
    specify that the lift setting should be determined at nominal operating 
    conditions and should be set at plus or minus 1% of the lift setting.
        For the second change, Surveillance Requirement 4.7.1.1 and Table 
    4.7-1 are modified to eliminate the need to verify the orifice size of 
    each MSSV.
        The third change modifies the statement for TS 3.7.1.1 so that if a 
    MSSV is inoperable and compensating action cannot be taken, the plant 
    must be brought to hot shutdown (Mode 4) within 12 hours instead of 
    cold shutdown (Mode 5) in 30 hours.
        Date of issuance: January 18, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 195
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 25, 1995 (60 FR 
    54723) The November 9, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated January 18, 1996. 
    No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    PECO Energy Company, Public Service Electric and Gas Company 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Docket Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station, Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 30, 1995
        Brief description of amendments: The amendments change the 
    technical specification requirements for control rod drive scram 
    accumulator and charging water header minimum pressure.
        Date of issuance: January 11, 1996
        Effective date: Unit 2, as of date of issuance, to be implemented 
    concurrently with Amendment 210, issued August 30, 1995; Unit 3, as of 
    date of issuance, to be implemented concurrently with Amendment 214, 
    issued August 30, 1995.
        Amendments Nos.: 211 and 216
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1995 (60 FR 
    63073) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 11, 1996 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Docket Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station, Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 21, 1995
        Brief description of amendments: The amendments change the test 
    pressure requirements for the high pressure coolant injection system 
    and the reactor core isolation cooling system surveillance tests. The 
    amendments also change Section 5.5.7 of the technical specifications to 
    eliminate reference to a section which was previously eliminated.
        Date of issuance: January 11, 1996
        Effective date: As of date of issuance.
        Amendments Nos.: 212 and 217
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 5, 1995 (60 FR 
    62271) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 11, 1996 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Docket Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station, Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: December 19, 1995
        Brief description of amendments: These amendments change the 
    ventilation filter test program bypass and penetration leakage test 
    acceptance criteria from less than 0.05 percent to less than 1.0 
    percent. The change corrects an administrative error that occurred 
    during the development of the Peach Bottom Improved Technical 
    Specifications which were issued as Amendments 210 and 214 to the Peach 
    Bottom licenses on August 30, 1995.
        Date of issuance: January 16, 1996
        Effective date: Unit 2, effective as of date of issuance, to be 
    implemented concurrently with Amendment 210, issued August 30, 1995; 
    Unit 3, effective as of date of issuance, to be implemented 
    concurrently with Amendment 214, issued August 30, 1995.
        Amendments Nos.: 213 and 218
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications. Public comments requested as to 
    proposed no significant hazards consideration: Yes (60 FR 66997, 
    December 27, 1995). That notice provided an opportunity to submit 
    comments on the Commission's proposed no significant hazards 
    
    [[Page 3508]]
    consideration determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by January 26, 
    1996, but indicated that if the Commission makes a final no significant 
    hazards consideration determination any such hearing would take place 
    after issuance of the amendment. The Commission's related evaluation of 
    the amendments, finding of exigent circumstances, and final 
    determination of no significant hazards consideration are contained in 
    a Safety Evaluation dated January 16, 1996
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
        Dated at Rockville, Maryland, this 23rd day of January 1996.
    
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation.
    [Doc. 96-1683 Filed 1-30-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Effective Date:
1/11/1996
Published:
01/31/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-20131
Dates:
January 11, 1996
Pages:
3497-3508 (12 pages)
PDF File:
x96-20131.pdf