X94-10105. Biweekly Notice Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 3 (Wednesday, January 5, 1994)]
    [Notices]
    [Pages 615-639]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-10105]
    
    
    [[Page Unknown]]
    
    [Federal Register: January 5, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
     
    
    Biweekly Notice Applications and Amendments to Facility Operating 
    Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from December 13, 1993, through December 22, 
    1993. The last biweekly notice was published on December 22, 1993 (58 
    FR 67840).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room P-223, Phillips Building, 7920 Norfolk Avenue, 
    Bethesda, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies 
    of written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By February 4, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, Unit 
    Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendment requests: December 2, 1993
        Description of amendment requests: The proposed changes would 
    modify TS 3/4.6.1.2 by removing the schedular requirements for a Type A 
    (overall integrated containment leakage rate) test to be performed 
    specifically at 40 1B 10 month intervals and replacing these 
    requirements with a requirement to perform Type A testing in accordance 
    with Appendix J to 10 CFR 50.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis about the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed changes would not involve an increase in the 
    probability or the consequences of an accident previously evaluated. 
    The proposed change only allows flexibility in the scheduling of the 
    three required Type A tests in the 10-year service period. The 
    additional flexibility is needed for plants using 18-month fuel 
    cycles to allow refueling outages and testing intervals to coincide. 
    There is no change to the number of tests required, test 
    methodology, or acceptance criteria.
        (2) The proposed changes would not create the possibility of a 
    new or different type of accident from any accident previously 
    evaluated. The proposed change to the test schedule only provides 
    flexibility in meeting the same requirement for three tests in a 10-
    year period. The testing type and bases have not changed. Therefore, 
    operation of the units with this more flexible test schedule will 
    not result in an accident previously not analyzed in the Updated 
    Final Safety Analysis Report (UFSAR). The proposed changes do not 
    impact the design bases of the containment and do not modify the 
    response of the containment during a design basis accident.
        (3) The proposed changes would not involve a reduction in the 
    margin of safety. The proposed changes to the schedule only provides 
    flexibility in meeting the same requirement for three tests in a 10-
    year period. These proposed changes do not affect or change any 
    limiting conditions for operation (LCO), or any other surveillance 
    requirements in the TS, and the basis for the surveillance 
    requirement remains unchanged. The testing method, acceptance 
    criteria, and bases are not changed. The TS continue to require 
    testing that is consistent with the requirements of Appendix J to 10 
    CFR 50.
        The NRC staff has reviewed the licensees' analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
        Attorney for licensees: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: Theodore R. Quay
    
    Gulf States Utilities Company, Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 18, 1993
        Description of amendment request: The proposed amendment would 
    permit extending the time to perform leak rate testing of certain 
    containment isolation valves so that the testing can be performed 
    during the refueling outage scheduled to start April 16, 1994, rather 
    than requiring an earlier shutdown solely to perform the testing. The 
    proposed amendment would revise Surveillance Requirements 4.6.1.3d and 
    4.6.1.3f to allow a one-time extension of the surveillance intervals 
    for leak rate testing of containment isolation valves. In addition, the 
    proposed amendment would revise Surveillance Requirements 4.4.3.2.2a 
    and 4.4.3.2.2b, replacing the requirement to leak test the reactor 
    coolant pressure isolation valves every 18 months or prior to returning 
    a valve to service, with a requirement to leak test the valves in 
    accordance with the Inservice Testing Program. This would allow the 
    testing to be performed during the fifth refueling outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
        1. The proposed changes would not significantly increase the 
    probability or consequences of a previously evaluated accident.
        One of the proposed technical specification (TS) changes requests a 
    one-time only extension of the surveillance intervals for the TS 
    Surveillance Requirements of TS 4.6.1.3f, leak rate testing of valves 
    sealed by the main steam positive leakage control system (MS-PLCS) and 
    the penetration valve leakage control system (PVLCS). The revision 
    would permit eleven containment isolation valves to be tested a maximum 
    of 46 days later than required by current technical specifications.
        To permit the one-time extension of the surveillance interval for 
    leak rate tests of containment isolation valves, TS 4.6.1.3d must also 
    be revised to permit the interval for Type C leak rate tests to exceed 
    24 months. This change is consistent with an associated exemption 
    request. The exemption request and this revision would permit 20 valves 
    to be tested a maximum of 35 days later than required by the current 
    technical specifications.
        The proposed amendment would also revise Surveillance Requirements 
    4.4.3.2.2a and 4.4.3.2.2b, replacing the requirement to leak test the 
    reactor coolant pressure isolation valves every 18 months or prior to 
    returning a valve to service, with a requirement to leak test the 
    valves in accordance with the Inservice Testing Program. This change 
    would require that the pressure isolation valves be tested in 
    accordance with Section XI of the ASME Boiler and Pressure Vessel Code, 
    resulting in the valves being tested at least every refueling outage, 
    rather than specifying an 18 month cycle. The revision would permit 
    five valves to be tested a maximum of 65 days later than allowed under 
    the current technical specification.
        Based on the short duration of the requested extensions, the 
    extensions will not significantly increase the probability or 
    consequences of a previously evaluated accident.
        2. The proposed changes would not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed TS changes permit extension of the surveillance 
    intervals for leak rate testing of containment isolation valves and 
    reactor coolant system pressure isolation valves. In that the requested 
    extension durations are small as compared to the overall interval 
    allowed by TS, the proposed changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        3. The proposed changes would not involve a significant reduction 
    in the margin of safety.
        The proposed TS changes permit extension of the surveillance 
    intervals for leak rate testing of containment isolation valves and 
    reactor coolant system pressure isolation valves. In that the requested 
    extension durations are small as compared to the overall interval 
    allowed by TS, the proposed changes do not involve a significant 
    reduction in the margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: Suzanne C. Black
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: December 8, 1993
        Description of amendments request: The frequency for Channel 
    Calibration would be revised from Q (quarterly) to R (refuel) for 
    Technical Specification Table 4.3.2.1, Item 4.a.4, High Pressure Core 
    Injection Steam Line Tunnel Temperature-High.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The proposed change corrects Technical 
    Specification pages issued for Amendment 166 for Brunswick Unit 1 
    and Amendment 197 for Brunswick Unit 2, regarding NUMAC Steam Leak 
    Detection Equipment. Specifically, on page 3/4 3-29 for each unit, 
    the Channel Calibration frequency of Item 4.a.4, HPCI [High Pressure 
    Core Injection] Steam Line Tunnel Temperature - High, was 
    inadvertently left as quarterly (Q) rather than being revised to 
    refuel (R). The text of CP&L's September 14, 1992 license amendment 
    request and the NRC's safety evaluation for Amendments 166 and 197, 
    dated October 14, 1993, addressed the frequency change from 
    quarterly to refuel for this item. Therefore, the proposed change is 
    purely administrative in nature and can not involve a significant 
    increase in the probability of consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. As stated above, the NRC's safety evaluation for 
    Amendments 166 and 197, dated October 14, 1993, addressed the 
    frequency change from quarterly to refuel for Item 4.a.4 of Table 
    4.3.2-1, HPCI Steam Line Tunnel Temperature - High. Therefore, the 
    proposed change is purely administrative in nature and can not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in the margin of safety. The proposed change corrects 
    Technical Specification pages issued for Amendment 166 for Brunswick 
    Unit 1 and Amendment 197 for Brunswick Unit 2, regarding NUMAC Steam 
    Leak Detection Equipment. The NRC's safety evaluation for Amendments 
    166 and 197, dated October 14, 1993, addressed the change of Channel 
    Calibration frequency of Item 4.a.4, HPCI Steam Line Tunnel 
    Temperature - High from quarterly (Q) to refuel (R). Therefore, the 
    proposed change is purely administrative and can not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: S. Singh Bajwa
    
    Dairyland Power Cooperative, Docket No. 50-409, La Crosse Boiling 
    Water Reactor (LACBWR), Vernon County, Wisconsin
    
        Date of application for amendment: November 5, 1993 (Reference LAC-
    13320)
        Brief description of amendment: This proposed change would modify 
    the Technical Specifications incorporated in Facility Operating License 
    No. DPR-45 in accordance with the requirements of the revised 10 CFR 
    Part 20 which becomes mandatory January 1, 1994 (56 FR 23360). In 
    addition, this proposed change would correct several editorial 
    oversights from previous amendments.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee provided 
    the results of its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the information provided by 
    the licensee and found that the licensee did not provide specific 
    information as to how it determined that the three standards of 
    50.92(c) were satisfied. The NRC staff performed its own evaluation of 
    the proposed change to determine if the three standards of 50.92(c) 
    were satisfied. The NRC staff's no significant hazards consideration 
    evaluation is presented below:
        1. Will operation of the facility according to this proposed change 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated?
        The proposed change is to bring the LACBWR Technical Specifications 
    into conformance with the revised 10 CFR Part 20 and to correct several 
    editorial oversights previously evaluated. The proposed change has no 
    affect on any plant operating parameters. Consequently, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Will operation of the facility according to this proposed change 
    create the possibility of a new or different kind of accident from any 
    previously evaluated?
        The proposed change is to bring the LACBWR Technical Specifications 
    into conformance with the revised 10 CFR Part 20 and to correct several 
    editorial oversights previously evaluated. The proposed change is 
    administrative in nature. Further, the proposed change does not result 
    in any physical alteration to any plant system, and does not result in 
    any change in the method by which any safety-related system performs 
    its function. Consequently, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Will operation of the facility according to this proposed change 
    involve a significant reduction in a margin of safety?
        The margin of safety is the difference between the value of a 
    critical design, operating, or post accident parameter, and the value 
    of the parameter which would produce unacceptable results. The proposed 
    change does not affect any hardware, has no effect on the current 
    operating methodologies or actions which govern plant performance, and 
    does not affect any accident analysis parameter. Consequently, the 
    proposed change does not involve a significant reduction in a margin of 
    safety.
        The NRC staff has determined based on its own no significant 
    hazards consideration evaluation that the three standards of 50.92(c) 
    are satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: La Crosse Public Library, 800 
    Main Street, La Crosse, Wisconsin 54601
        Attorney for licensee: Fritz Schubert, Esquire, Dairyland Power 
    Cooperative, 2615 East Avenue South, La Crosse, Wisconsin 54601
        NRC Branch Chief: John H. Austin
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: November 11, 1993
        Description of amendment request: The proposed amendments would 
    consolidate the Quality Verification Department with the Nuclear 
    Generation Department and realign the Nuclear Safety Review Board such 
    that it reports to the Senior Vice-President of the Nuclear Generation 
    Department.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        [1. The amendments do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.]
        The proposed revisions to consolidate the Quality Verification 
    Department with the Nuclear Generation Department and realign the 
    NSRB [Nuclear Safety Review Board] such that it reports to the 
    Senior Nuclear Officer, change the reference from Semiannual to 
    Annual, change the reference from group to division, delete titles 
    of persons designated to approve modifications, clarify the 
    responsibilities of the Safety Assurance Manager, and delete the 
    requirement to perform an annual independent Fire Protection Audit 
    will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated because the changes 
    do not have any impact upon the design or operation of any plant 
    systems or components.
        [2. The amendments do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.]
        The proposed revisions will not create the possibility of a new 
    or different kind of accident from any previously evaluated because 
    the changes are administrative in nature and operation of Catawba, 
    McGuire, and Oconee Nuclear Stations in accordance with these TS 
    [technical specifications] will not create any failure modes not 
    bounded by previously evaluated accidents.
        [3. The amendments do not involve a significant reduction in a 
    margin of safety.]
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Loren R. Plisco, Acting
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: November 11, 1993
        Description of amendment request: The proposed amendments would 
    consolidate the Quality Verification Department with the Nuclear 
    Generation Department and realign the Nuclear Safety Review Board such 
    that it reports to the Senior Vice-President of the Nuclear Generation 
    Department.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        [1. The amendments do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.]
        The proposed revisions to consolidate the Quality Verification 
    Department with the Nuclear Generation Department and realign the 
    NSRB [Nuclear Safety Review Board] such that it reports to the 
    Senior Nuclear Officer, change the reference from Semiannual to 
    Annual, change the reference from group to division, delete titles 
    of persons designated to approve modifications, clarify the 
    responsibilities of the Safety Assurance Manager, and delete the 
    requirement to perform an annual independent Fire Protection Audit 
    will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated because the changes 
    do not have any impact upon the design or operation of any plant 
    systems or components.
        [2. The amendments do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.]
        The proposed revisions will not create the possibility of a new 
    or different kind of accident from any previously evaluated because 
    the changes are administrative in nature and operation of Catawba, 
    McGuire, and Oconee Nuclear Stations in accordance with these TS 
    [technical specifications] will not create any failure modes not 
    bounded by previously evaluated accidents.
        [3. The amendments do not involve a significant reduction in a 
    margin of safety.]
        The proposed revisions will not involve a reduction in a margin 
    of safety because they are administrative in nature.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Loren R. Plisco, Acting
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: November 11, 1993
        Description of amendment request: The proposed amendments would 
    consolidate the Quality Verification Department with the Nuclear 
    Generation Department and realign the Nuclear Safety Review Board such 
    that it reports to the Senior Vice-President of the Nuclear Generation 
    Department. In addition, the requirement to conduct an annual 
    independent Fire Protection Audit is deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        [1. The amendments do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.]
        The proposed revisions to consolidate the Quality Verification 
    Department with the Nuclear Generation Department and realign the 
    NSRB [Nuclear Safety Review Board] such that it reports to the 
    Senior Nuclear Officer, change the reference from Semiannual to 
    Annual, change the reference from group to division, delete titles 
    of persons designated to approve modifications, clarify the 
    responsibilities of the Safety Assurance Manager, and delete the 
    requirement to perform an annual independent Fire Protection Audit 
    will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated because the changes 
    do not have any impact upon the design or operation of any plant 
    systems or components.
        [2. The amendments do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.]
        The proposed revisions will not create the possibility of a new 
    or different kind of accident from any previously evaluated because 
    the changes are administrative in nature and operation of Catawba, 
    McGuire, and Oconee Nuclear Stations in accordance with these TS 
    [technical specifications] will not create any failure modes not 
    bounded by previously evaluated accidents.
        [3. The amendments do not involve a significant reduction in a 
    margin of safety.]
        The proposed revisions will not involve a reduction in a margin 
    of safety because they are administrative in nature.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Loren R. Plisco, Acting
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: November 16, 1993
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to change the periodic test 
    schedule for containment Type A integrated leak rate tests (ILRTs) from 
    a set of three tests performed at approximately equal intervals during 
    each 10-year period, as specified in 10 CFR Part 50, Appendix J, 
    Section III.D, to one Type A test performed at 10-year intervals. The 
    change is being reviewed in conjunction with a proposed exemption to 
    Appendix J, as requested by the licensee in a letter dated November 16, 
    1993.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The Waterford 3 Type A test history provides substantial 
    justification for the proposed test schedule. Three type A tests 
    have been performed over an eight (8) year period with successful 
    results. The tests indicate that Waterford 3 has a low leakage 
    containment and that the leakage has never exceeded 24.6% of 
    La. [La is the maximum allowed leakage rate of air from 
    containment where containment is pressurized to Pa; for 
    Waterford 3 Pa is 44 psig. La for Waterford is 0.50 
    percent by weight of the containment air per 24 hours at Pa.]
        There are no structural mechanisms which would adversely affect 
    the structural capability of the containment and that would be a 
    factor in extending the Type A test schedule to ten years. A risk 
    impact assessment was performed, and a determination was made that 
    there is no risk impact as a result of changing the Type A test 
    schedule. Therefore, the proposed change will not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated.
        There are no design changes being made that would create a new 
    type of accident or malfunction. The proposed change will not alter 
    the plant or the manner in which it is operated. The change proposes 
    a change to the schedule for performing the periodic Type A test. 
    The purpose of the test is to provide periodic verification by test 
    of the leaktight integrity of the primary reactor containment, and 
    systems and components which penetrate containment. The tests assure 
    that leakage through containment and systems and components 
    penetrating containment will not exceed the allowable leakage rate 
    values associated with conditions resulting from an accident. The 
    change in schedule for performing the Type A test will not adversely 
    affect the containment integrity in the event of an accident. 
    Therefore, the proposed change will not create the possibility of a 
    new or different type of accident from any accident previously 
    evaluated.
        The proposed change is a change to the schedule for performing 
    the periodic Type A tests and does not reduce the margin of safety 
    assumed in accident analysis for release of radioactive materials 
    from the containment atmosphere into the environment or any margin 
    of safety preserved by the Technical Specifications. The 
    methodology, acceptance criteria, and the technical specification 
    leakage limits for the performance of the Type A tests will not 
    change, and the Type A tests will be performed in accordance with 
    10CFR 50, Appendix J, and the Waterford 3 licensing basis. 
    Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: November 16, 1993
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TSs) to provide acceptable 
    conditions for operation when (1) the core operating limits supervisory 
    system (COLSS) is in service and neither control element assembly 
    calculator (CEAC) is operable and (2) the COLSS is out of service and 
    either or both CEACs are operable.
        This proposed TS change modifies the departure from nucleate 
    boiling ratio (DNBR) margin, Limiting Condition for Operation (LCO) 
    3.2.4b and c, which limits the core power distribution to the initial 
    value assumed in the accident analyses. Operation within this LCO 
    either limits or prevents potential fuel cladding failures in the event 
    of a postulated accident and limits damage to the fuel cladding during 
    an accident by ensuring that the plant is operating within acceptable 
    conditions at the onset of a transient. The limiting safety system 
    settings and this LCO are based on the accident analysis, so that 
    specified acceptable fuel design limits (SAFDLs) are not exceeded as a 
    result of anticipated operational occurrences (AOOs) and the limits of 
    acceptable consequences are not exceeded for other postulated 
    accidents.
        The COLSS and core protection calculators (CPCs) monitor the core 
    power distribution on line and are capable of verifying that the linear 
    heat rate (LHR) and DNBR do not exceed their limits. The COLSS performs 
    this function by continuously monitoring the core power distribution 
    and calculating core power operating limits corresponding to the 
    allowable peak LHR and DNBR. The CPCs perform this function by 
    continuously calculating an actual value of DNBR and LHR for comparison 
    with the respective trip setpoints. CEACs monitor CEA position. Should 
    a CEA deviate from its subgroup position, the CEACs will transmit an 
    appropriate ``penalty'' factor to the CPCs.
        The COLSS is normally used to monitor DNBR margin. When at least 
    one CEAC is operable, TS 3.2.4a provides enough margin to DNB to 
    accommodate the limiting AOO without failing the fuel. When neither 
    CEAC is operable, the CPCs lack the CEA position information necessary 
    to ensure a reactor trip when necessary. In this case TS 3.2.4b 
    requires the COLSS calculated core power to be reduced to ensure that 
    the limiting AOO will not result in fuel failure. Currently, TS 3.2.4b 
    requires that the COLSS calculated power be maintained at 13% below the 
    COLSS calculated power operating limit to compensate for the potential 
    error in the CPC DNBR calculation. The proposed revision would increase 
    this required adjustment to 16%, which is more restrictive than the 
    present value.
        In instances when the COLSS is out of service, but either or both 
    CEACs are operable, TS 3.2.4c states that the DNBR operating margin 
    shall be maintained by comparing the DNBR indicated on any operable CPC 
    channel with the allowable value from TS Figure 3.2-2. Whenever the 
    COLSS is out of service, the CPCs are used to perform the same 
    monitoring function. However, the extra conservatisms built into the 
    CPCs for transient protection are not all required when the CPCs are 
    being used for monitoring. In order not to affect the CPC transient 
    protection, these conservatisms are not taken from the CPC, but are 
    credited in the COLSS out-of-service limits in Figure 3.2-2. A 
    reevaluation of the limiting AOOs has verified that, by maintaining the 
    margin in the proposed Figure 3.2-2, sufficient margin exists to ensure 
    that the limiting Cycle 7 AOO will not result in fuel failure.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        For the case when neither CEAC is operable but COLSS is in 
    service, the CPCs assume a preset CEA configuration and can not 
    obtain the required CEA position information to ensure the SAFDL on 
    DNBR will not be violated during an AOO. Thus, as a result of 
    limiting AOOs for Cycle 7, Specification 3.2.4b requires that core 
    power be reduced to a value 16% less than the current COLSS 
    calculated power operating limit. This ensures the limiting AOO will 
    not result in a violation of SAFDLs. The proposed revision to Figure 
    3.2-2 accounts for the situation when COLSS is out of service but at 
    least one CEAC is operable. In this case, the Cycle 7 safety 
    analysis has shown that by maintaining the CPC calculated DNBR above 
    the value shown in the figure, the limiting AOO will not result in a 
    violation of the SAFDLs. Therefore, the proposed change will not 
    significantly increase the probability or consequences of any 
    accident previously evaluated.
        The proposed changes are primarily a result of changes in Cycle 
    7 core parameters. These changes do not involve any change to any 
    equipment or manner in which the plant will be operated. These 
    changes further restrict the plant operation when either COLSS or 
    both CEACs are out of service. Therefore, the proposed change will 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The intent of this Specification is to ensure that there is 
    always sufficient margin to DNB such that the CPCs can mitigate the 
    consequences of the most limiting AOO prior to a violation of the 
    SAFDLs. Generally, this margin is continuously monitored by COLSS; 
    however, if COLSS is out of service, but at least one CEAC is 
    operable, the limitation on CPC calculated DNBR (as a function of 
    ASI [axial shape index]) shown in Figure 3.2-2 represents a 
    conservative envelope of operating conditions consistent with the 
    Cycle 7 safety analysis assumptions. This band of operating 
    conditions has been analytically demonstrated to maintain an 
    acceptable minimum DNBR through all AOOs. On the other hand, for the 
    case when COLSS is in service, but neither CEAC is operable, the 
    proposed change will ensure that the limiting AOO will not result in 
    a violation of SAFDLs. Therefore, the proposed changes will not 
    result in a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: December 2, 1993
        Description of amendment request: The purpose of the request is to 
    change the plant Technical Specifications (TS) to remove the limiting 
    conditions for operation and surveillance requirements for the chlorine 
    detection system. TMI-1 removed the gases Chlorination System for the 
    Circulating Water and River Water Systems. This modification eliminated 
    the need for a Chlorine Dectection System (CDS).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated. The TS requirements assured the operability of 
    the CDS in the event of an on-site chlorine release from a one ton 
    cylinder. These TS requirements reduced the probability and the 
    consequences of a radiological accident which may result from an 
    incapacitation of control room operatorsafter entry of chlorine into 
    the control room. With the removal and the restriction on delivery 
    of one ton chlorine cylinders, this postulated event is no longer 
    credible, and there is a decrease in the probability of a 
    radiological accident.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The TS 
    requirements associated with the CDS were for the on-site release of 
    chlorine from a one ton cylinder. These cylinders are removed and 
    prohibited from the TMI-1 site. These actions preclude a significant 
    on-site release of chlorine which could affect the control room 
    operators.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety. The purpose of the TS requirements was to maintain 
    operability of the CDS in the event of on-site release from a one 
    ton chlorine cylinder. Since chlorine cylinders greater than 150 
    pounds are prohibited on-site, the TS requirements for chlorine 
    detection are no longer required, and their removal will not reduce 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: November 23, 1993
        Description of amendment request: The licensee proposes to modify 
    the South Texas Project, Units 1 and 2, Technical Specification 3/
    4.8.1.1, ``A.C. Sources,'' to modify the action statements and 
    surveillance requirements for testing of the standby diesel generator. 
    This amendment would incorporate the recommendations of NRC Generic 
    Letter (GL) 93-05, ``Line-Item Technical Specifications Improvements To 
    Reduce Surveillance Requirements For Testing During Power Operation,'' 
    dated September 27, 1993.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change seeks to eliminate the unnecessary testing 
    of an operable Standby Diesel Generator (SDG). Technical 
    Specification (TS) 3.8.1.1 Actions a. and e. require all operable 
    SDGs be started as a demonstration of operability whenever one or 
    more of the offsite AC [alternating current] power sources is 
    declared inoperable. The inoperability of an offsite AC power source 
    has no effect on the reliability of a SDG. Deleting this requirement 
    does not affect the design or performance characteristics of the 
    SDGs. Therefore, the SDGs maintain their ability to perform their 
    design function.
        TS 3.8.1.1 Actions b. and c. require all remaining operable SDGs 
    be started as a demonstration of operability whenever one of the SDG 
    is declared inoperable except for preplanned preventive maintenance 
    or testing. The proposed amendment would expand the testing 
    exclusion to include an inoperable support system and an 
    independently testable component in addition to preplanned 
    preventive maintenance and testing. The proposed amendment would 
    also eliminate the testing requirement of the remaining operable 
    SDGs, when a SDG is declared inoperable, unless there is cause to 
    believe a potential common mode failure exists for the remaining 
    SDGs. The normal TS surveillance testing schedule assures that 
    operable SDG(s) are capable of performing their intended safety 
    functions. A failure of one SDG does not reduce the reliability of 
    another, otherwise operable SDG. Deleting this requirement does not 
    affect the design or performance characteristics of the SDGs, once a 
    common mode failure has been dismissed. Therefore, the SDGs maintain 
    their ability to perform their design function.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The elimination of these unnecessary tests does not affect the 
    design bases of the SDGs, or any of the accident evaluations 
    involving the SDGs. The SDGs are designed to provide electrical 
    power to the equipment important for safety during all modes and 
    plant conditions following a loss of offsite power. The test 
    schedule established in accordance with GL 84-15 [``Proposed Staff 
    Actions To Improve and Maintain Diesel Generator Reliability''] 
    assures that operable SDGs are capable of performing their intended 
    safety function. Therefore, this change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        Since the proposed change does not affect the design bases, 
    accident analysis, reliability or capability of the SDGs to perform 
    their intended safety function, this change does not involve any 
    reduction in a margin to safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton Texas 77488
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, NW, Washington, DC 20036
        NRC Project Director: Suzanne C. Black
    
    Indiana Michigan Power Company, Docket No. 50-315, Donald C. Cook 
    Nuclear Plant, Unit No. 1, Berrien County, Michigan
    
        Date of amendment request: December 15, 1993. This submittal 
    supersedes a previous submittal dated March 10, 1993.
        Description of amendment request: The proposed amendment would 
    implement interim tube plugging criteria for the tube support plate 
    elevation outer diameter stress corrosion cracking for cycle 14.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of Donald C. Cook Nuclear Plant Unit 1 in 
    accordance with the proposed license amendment does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        Testing of model boiler specimens for free span tubing (no TSP 
    restraint) at room temperature conditions shows burst pressures in 
    excess of 5000 psi for indications of ODSCC with voltage 
    measurements as high as 19 volts. Burst testing performed on pulled 
    tubes from Cook Nuclear Plant Unit 1 with up to a 2.02 volt 
    indication shows measured burst in excess of 10,000 psi at room 
    temperature. Correcting for the effects of temperature on material 
    properties and minimum strength levels (as the burst testing was 
    done at room temperature), tube burst capability significantly 
    exceeds the RG 1.121 criterion requiring the maintenance of a margin 
    of 3 times normal operating pressure differential on tube burst. The 
    3 times normal operating pressure differential for the Cook Nuclear 
    Plant Unit 1 steam generators corresponds to 4275 psi. Based on the 
    existing data base, this criterion is satisfied with 7/8'' diameter 
    tubing with bobbin coil indications with signal amplitudes less than 
    4.9 volts, regardless of the indicated depth measurement. A 1.0 volt 
    plugging criteria compares favorably with the structural limit 
    considering the previously calculated growth rates for ODSCC within 
    the Cook Nuclear Plant Unit 1 steam generators. Considering a 
    voltage increase of 0.4 volts, and adding a 20% NDE uncertainty of 
    0.20 volts (90% Cumulative Probability) to the IPC of 1.0 volts 
    results in an EOC voltage of approximately 1.6 volts for Cycle 14 
    operation. A 3.3 volt safety margins implied (4.9 structural limit - 
    1.6 volt EOC - 3.3 volt margin). This EOC voltage compares favorably 
    with the Structural Limit of 4.9 volts.
        For the voltage/burst correlation, the EOC structural limit is 
    supported by a voltage of 4.9 volts. A 3.1 volt BOC repair limit 
    confirms the structural limit when 40% growth and 20% uncertainty 
    are applied to the repair limit. This repair limit will be applied 
    for Cycle 14 IPC implementation to repair bobbin indication greater 
    than 3.1 volts independent of RPC confirmation of the indication.
        The conservatism of this repair limit is shown by the EOC 12 
    (Summer 1992) eddy current data. The overall average voltage growth 
    was determined to be only 2.2%, with a 12% average voltage growth 
    for indications less than 0.75 volt BOC and a 1% average voltage 
    growth for indication >0.75 volt at the BOC. In addition, the Cycle 
    12 maximum observed voltage increase was found to be 0.49 volts, and 
    occurred in a tube initially <1.0 boc.="" in="" accordance="" with="" the="" technical="" specification="" requirements,="" the="" applicability="" of="" cycle="" 13="" growth="" rates="" for="" cycle="" 14="" operation="" will="" be="" confirmed="" prior="" to="" return="" to="" power="" of="" cook="" nuclear="" plant="" unit="" 1.="" similar="" large="" structural="" margins="" are="" anticipated.="" as="" stated="" previously,="" tsp="" proximity="" to="" the="" tubes="" will="" prevent="" tube="" burst="" during="" all="" plant="" conditions.="" test="" data="" indicates="" that="" tube="" burst="" cannot="" occur="" within="" the="" tsp,="" even="" for="" tubes="" which="" have="" 100%="" through-wall="" edm="" notches,="" 0.75="" inch="" long,="" provided="" that="" the="" tsp="" is="" adjacent="" to="" the="" notched="" area.="" therefore,="" a="" more="" realistic="" assessment="" of="" tube="" operability="" should="" be="" performed="" against="" the="" rg="" 1.121="" loading="" requirements="" during="" accidents="" slb="" conditions,="" since="" the="" tsp="" has="" the="" potential="" to="" deflect="" during="" blowdown="" following="" a="" main="" slb,="" thereby="" uncovering="" the="" intersection.="" at="" the="" asme="" code="" recommended="" faulted="" condition="" loading="" of="" 3657="" psi="" (2560="" psi/0.7)="" structural="" integrity="" is="" provided="" for="" bobbin="" voltage="" indications="" of="" a="" minimum="" of="" 9.6="" volts.="" the="" repair="" limit="" based="" on="" the="" structural="" limited="" conservative="" slb="" conditions="" would="" be="" 6.0="" volts="" (compared="" to="" a="" 3.1="" volt="" repair="" limit="" for="" a="" structural="" limit="" based="" on="" the="" 3[delta]p="" burst="" capability="" voltage).="" only="" three="" indications="" of="" odscc="" have="" been="" reported="" to="" have="" operating="" leakage,="" and="" all="" three="" have="" been="" in="" european="" plants.="" no="" field="" leakage="" has="" been="" reported="" at="" other="" plants="" from="" tubes="" with="" indications="" of="" a="" voltage="" level="" of="" under="" 7.7="" volts="" (from="" 3/4''="" tubing).="" relative="" to="" the="" expected="" leakage="" during="" accident="" condition="" loadings,="" it="" has="" been="" previously="" established="" that="" a="" postulated="" main="" slb="" outside="" of="" containment="" but="" upstream="" of="" the="" msiv="" represents="" the="" most="" limiting="" radiological="" condition="" relative="" to="" the="" ipc.="" in="" support="" of="" implementation="" of="" the="" ipc,="" it="" will="" be="" determined="" whether="" the="" distribution="" of="" cracking="" indications="" at="" the="" tsp="" intersections="" at="" the="" eoc="" 14="" are="" projected="" to="" be="" such="" that="" primary="" to="" secondary="" leakage="" would="" result="" in="" site="" boundary="" doses="" within="" a="" small="" fraction="" of="" the="" 10="" cfr="" 100="" guidelines.="" the="" slb="" leakage="" rate="" calculation="" methodology="" prescribed="" in="" section="" 3.3="" of="" draft="" nureg-1477="" will="" be="" used="" to="" calculate="" eoc="" 14="" leakage.="" due="" to="" the="" relatively="" low="" voltage="" growth="" rates="" at="" cook="" nuclear="" plant="" unit="" 1="" and="" the="" relatively="" small="" number="" of="" indications="" affected="" by="" the="" ipc,="" slb="" leakage="" prediction="" per="" draft="" nureg-1477="" is="" expected="" to="" be="" less="" than="" the="" acceptance="" limit="" of="" 1.0="" gpm="" in="" the="" faulted="" loop="" and="" far="" below="" the="" conservatively="" calculated="" srp="" based="" allowable="" value="" of="" 120="" gpm="" in="" the="" faulted="" loop.="" the="" nrc="" leakage="" rate="" calculation="" methodology="" applies="" a="" 98%="" confidence="" limit="" on="" leakage="" that="" is="" independent="" of="" voltage.="" this="" method="" for="" calculating="" slb="" leakage="" is="" conservative="" as="" it="" assumes="" no="" correlations="" exists="" between="" slb="" leakage="" and="" bobbin="" probe="" voltage.="" tube="" pull="" results="" from="" cook="" nuclear="" plant="" unit="" 1="" indicate="" that="" tube="" wall="" degradation="" of="" greater="" than="" 40%="" through-wall="" was="" detectable="" either="" by="" the="" bobbin="" or="" rpc="" probe.="" the="" tube="" with="" maximum="" through-="" wall="" penetration="" of="" 56%="" (42%="" average)="" had="" a="" voltage="" of="" 2.02="" volts.="" this="" indication="" also="" was="" the="" largest="" recorded="" bobbin="" voltage="" from="" the="" eoc="" 12="" eddy="" current="" data.="" all="" burst="" tested="" tube="" intersections="" had="" degradation="" depths="" of="" 40%="" to="" 56="" %="" (actual)="" deep="" and="" all="" were="" detected="" by="" both="" probes,="" with="" all="" bobbin="" voltage="" grater="" than="" or="" equal="" to="" 1.0.="" since="" the="" criteria="" requires="" the="" plugging="" of="">1.0 volt 
    bobbin indications with confirmed RPC calls, using the Cook Nuclear 
    Plant Unit 1 pulled tube destructive examination results, it is 
    reasonable that no indications of degradation greater than 40% to 
    56% deep with an ability to influence tube burst capability were 
    left in service. Since the majority of the EOC 14 indications at 
    Cook Nuclear Unit 1 are expected to be below this level, the 
    inclusion of all IPC intersections into the leakage calculation is 
    exceptionally conservative.
        Therefore, as re-implementation of the 1.0 volt IPC during Cycle 
    14 does not adversely affect steam generator tube integrity and 
    results in acceptable dose consequences, the proposed amendment does 
    not result in any increase in the probability or consequences of an 
    accident previously evaluated within the Cook Nuclear Plant Unit 1 
    FSAR.
        2. The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Implementation of the proposed steam generator tube IPC does not 
    introduce any significant changes to the plant design basis. Use of 
    the criteria does not provide a mechanism which could result in a 
    tube rupture outside of the region of the TSP elevations; no ODSCC 
    is occurring outside the thickness of the TSPs. Neither a single or 
    multiple tube rupture event would be expected in a steam generator 
    in which the plugging criteria has been applied (during all plant 
    conditions).
        Specifically, Cook Nuclear Plant will continue to implement a 
    maximum leakage rate limit of 150 gpd (0.1 gpm) per steam generator 
    to help preclude the potential for excessive leakage during all 
    plant conditions. The Cycle 14 Technical Specification limits on 
    primary to secondary leakage at operating conditions is a maximum of 
    0.4 gpm (600 gpd) for all steam generators, or, a maximum of 150 gpd 
    for any one steam generator. The RG 1.121 criterion for establishing 
    operational leakage rate limits that require plant shutdown are 
    based upon leaks-before-break consideration to detect a free span 
    crack before potential tube rupture. The 150 gpd limit should 
    provide for leakage detection and plant shutdown in the event of the 
    occurrence of an unexpected single crack resulting in leakage that 
    is associated with the longest permissible crack length. RG 1.121 
    acceptance criteria for establishing operating leakage limits are 
    based on leak-before-break considerations such that plant shutdown 
    is initiated if the leakage associated with the longest permissible 
    crack is exceeded. The longest permissible crack is the length that 
    provides a safety factor of 3 against bursting at normal operating 
    pressure differential. A voltage amplitude of 4.9 volts for typical 
    ODSCC corresponds to meeting this tube burst requirement at a lower 
    95% prediction limit on the burst correlation coupled with 95/95 LTL 
    material properties. Alternate crack morphologies can correspond to 
    4.9 volts so that a unique crack length is not defied by the burst 
    pressure versus voltage correlation. Consequently, typical burst 
    pressure versus through-wall crack length correlations are used 
    below to define the ``longest permissible crack'' for evaluating 
    operating leakage limits.
        At current plant conditions, the single through-wall crack 
    lengths that result in tube burst at 3 times normal operating 
    pressure differential and SLB conditions are 0.44 inch and 0.84 
    inch, respectively. A leak rate of 150 gpd will provide for 
    detection of 0.42 inch long cracks at nominal leak rates and 0.61 
    inch long cracks at the lower 95% confidence level leak rates. Since 
    tube burst is precluded during normal operation due to the proximity 
    of the TSP to the tube and the potential for the crevice to become 
    uncovered during SLB conditions, the leakage from the maximum 
    permissible crack must preclude tube burst at SLB conditions. Thus, 
    the 150 gpd limit provides for plant shutdown prior to reaching 
    critical crack lengths for SLB conditions.
        3. The proposed license amendment does not involve a significant 
    reduction in margin of safety.
        The use of the voltage based bobbin probe interim TSP elevation 
    plugging criteria at Cook Nuclear Plant Unit 1 is demonstrated to 
    maintain steam generator tube integrity commensurate with the 
    criteria of Regulatory Guide 1.121. RG 1.121 describes a method 
    acceptable to the NRC staff for meeting GDCs 14, 15, 31, and 32 by 
    reducing the probability or the consequences of steam generator tube 
    rupture. This is accomplished by determining the limiting conditions 
    of degradation of steam generator tubing, as established by 
    inservice inspection, for which tubes with unacceptable cracking 
    should be removed from service. Upon implementation of the criteria, 
    even under the worst case conditions, the occurrence of ODSCC at the 
    TSP elevations is not expected to lead to a steam generator tube 
    rupture event during normal or faulted plant conditions. The EOC 14 
    distribution of crack indications at the TSP elevations will be 
    confirmed to result in acceptable primary to secondary leakage 
    during all plant conditions and that radiological consequences are 
    not adversely impacted.
        In addressing the combined effects of LOCA + SSE on the steam 
    generator component (as required by GDC 2), it has been determined 
    that tube collapse may occur in the steam generators at some plants. 
    This is the case as the TSPs may become deformed as a result of 
    lateral loads at the wedge supports at the periphery of the plant 
    due to the combined effects of the LOCA rarefaction wave and SSE 
    loadings. Then, the resulting pressure differential on the deformed 
    tubes may cause some of the tubes to collapse.
        There are two issues associated with steam generator tube 
    collapse. First, the collapse of steam generator tubing reduces the 
    RCS flow area through the tubes. The reduction in flow are increases 
    the resistance to flow of steam from the core during a LOCA which, 
    in turn, may potentially increase peak clad temperature (PCT). 
    Second, there is a potential that partial through-wall cracks in 
    tubes could progress to through-wall cracks during tube deformation 
    or collapse.
        Consequently, since the leak-before-break methodology is 
    applicable to the Cook Nuclear Plant Unit 1 reactor coolant loop 
    piping, the probability of breaks in the primary loop piping is 
    sufficiently low that they need not be considered in the structural 
    design of the plant. The limiting LOCA event becomes either the 
    accumulator line brake or the pressurizer surge line break. LOCA 
    loads for the primary pipe breaks were used to bound the Cook 
    Nuclear Plant Unit 1 smaller breaks. The results of the analysis 
    using the larger break inputs show that the LOCA loads were found to 
    be of insufficient magnitude to result in steam generator tube 
    collapse or significant deformation.
        Addressing RG 1.83 consideration, implementation of the bobbin 
    probe voltage based interim tube plugging criteria of 1.0 volt is 
    supplemented by the following: enhanced eddy current inspection 
    guidelines to proved consistency in voltage normalization, a 100% 
    eddy current inspection sample size at the TSP elevations, and RPC 
    inspection requirements as outlined in the technical specifications 
    and Appendix A ``NDE Data Acquisition and Analysis Guidelines'' 
    (Attachment 6).
        As noted previously, implementation of the TSP elevation 
    plugging criteria will decrease the number of tubes which must be 
    repaired. The installation of steam generator tube plugs reduce the 
    RCS flow margin. Thus, implementation of the alternate plugging 
    criteria will maintain the margin of flow that would otherwise be 
    reduced in the event of increased tube plugging.
        Based on the above, it is concluded that the proposed license 
    amendment request does not result in a significant reduction in 
    margin with respect to plant safety as defined in the Final Safety 
    Analysis Report or any of the plant Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Leaks Preston Palenske 
    Memorial Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: A Randolph Blough, Acting
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of amendment requests: November 15, 1993
        Description of amendment requests: The proposed amendments delete 
    certain Limiting Conditions for Operation, Actions, and Surveillance 
    Requirements for Reactor Coolant System Pressure Isolation Valves in 
    the Technical Specifications. The Technical Specifications for these 
    Reactor Coolant System Pressure Isolation Valves were added by Order 
    dated April 20, 1981. This Order was prompted by concerns for an 
    interfacing system loss-of-coolant accident as identified in the 
    Reactor Safety Study (WASH-1400). The proposed Technical Specification 
    change, by inference, also requests rescission of the April 20, 1981 
    Order.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Per 10 CFR 50.92, a proposed amendment to an operating license 
    will not involve a significant hazards consideration if the proposed 
    amendment satisfies the following three criteria:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously analyzed,
        2. Does not create the possibility of a new or different kind of 
    accident from an accident previously analyzed or evaluated, or
        3. Does not involve a significant reduction in a margin of 
    safety.
        Criterion 1
        The ISLOCA is not one of the accidents previously analyzed in 
    Chapter 14, Safety Analysis, of the Cook Nuclear Plant Updated Final 
    Safety Analysis Report. Chapter 14 analyzes the large break LOCA in 
    Section 14.3.1, and ``loss of reactor coolant from small ruptured 
    pipes or from cracks in large pipes which actuates the ECCS'', or 
    small break LOCA in Section 14.3.2. Therefore, deleting from the 
    Technical Specifications the Reactor Coolant System pressure 
    isolation valves in Table 3.4-0, will not increase the probability 
    or the consequences of the large break or the small break LOCAs 
    previously analyzed for the Cook Nuclear Plant.
        Criterion 2
        The Reactor Coolant System pressure isolation valves in Table 
    3.4-0 of the Technical Specifications were added because WASH-1400 
    identified the ISLOCA as a significant contributor to core damage 
    frequency. Deletion of the subject valves from the Technical 
    Specifications and reliance on the testing requirements mandated by 
    the In-Service Testing Program of ASME XI does not create the 
    possibility of a new or different kind of accident from the large 
    break or the small break LOCAs previously analyzed for the Cook 
    Nuclear Plant.
        Criterion 3
        Deleting the Reactor Coolant System pressure isolation valves 
    from the testing requirements in Table 3.4-0 of the Technical 
    Specifications will result in these valves only being tested on a 
    refueling outage frequency as part of the ASME B&PV Code Section XI 
    IST Program. This somewhat reduced testing frequency will result in 
    a slight increase in the ISLOCA contribution to core damage 
    frequency of 5.4%, from lower 5.00E-08/reactor year to mid 5.00E-08/
    reactor year. This insignificant increase will not affect the 
    overall core damage frequency of 6.26E-05/reactor year. Therefore, 
    it is concluded that the proposed deletion of the Reactor Coolant 
    System pressure isolation valves in Table 3.4-0 of the Technical 
    Specifications, as well as the proposed deletion of the portions of 
    the Technical Specifications that are affected by Table 3.4-0, will 
    not result in a significant reduction in the margin of safety that 
    exists at Cook Nuclear Plant to prevent an ISLOCA or to mitigate the 
    consequences of an ISLOCA.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: A. Randolph Blough, Acting
    
    Pacific Gas and Electric Company, Docket No. 50-133, Humboldt Bay 
    Power Plant, Unit 3, Humboldt County, California
    
        Date of application for amendment: October 8, 1993 (Reference LAR 
    93-02)
        Brief description of amendment: This Licensee Amendment Request 
    (LAR) proposes to revise the Humboldt Bay Power Plant (HBPP), Unit 3, 
    Technical Specifications (TS) by deleting Figure II-2 in Section II, 
    ``Site,'' by deleting the Restricted Area boundary line in Figure V-3, 
    Section V, ``Monitoring Systems,'' by incorporating a title change into 
    Section VII, ``Administrative Controls,'' and by revising Figure VII-2, 
    ``Plant Staff Organization.'' The proposed changes are in response to 
    the revised 10 CFR Part 20 which becomes mandatory on January 1, 1994 
    (56 FR 23360). The specific TS changes proposed are as follows:
        (1) Page v, Figures - delete reference to Figure II-2.
        (2) Page II-1, Section II.B, Plant Areas - change ``is shown in 
    Figure II-2'' to ``shall be defined in plant procedures.''
        (3) Page II-3, Section II - delete Figure II-2.
        (4) Page V-14, Section V - delete the Restricted Area boundary line 
    from Figure V-3, ``HBPP Groundwater Monitoring Systems Wells,'' to be 
    consistent with item 3 above.
        (5) Page VII-5, Section VII.C.2.e, Supervisor of Maintenance - 
    change the title from ``Supervisor of Maintenance'' to ``Maintenance 
    Planner.''
        (6) Page VII-10, Section VII.D.1.b., Membership, List of minimum 
    membership - replace ``Supervisor of Maintenance'' with ``Maintenance 
    Planner.''
        (7) Page VII-31, Section VII, Figure VII-2, Plant Staff 
    Organization - replace ``Maintenance Supervisor'' with ``Maintenance 
    Planner.''
        (8) Page VII-31, Section VII, Figure VII-2, Plant Staff 
    Organization - both the Mechanical Foreman and the Instrument/
    Electrical Foreman report directly to the Plant Manager, not to the 
    ``Maintenance Planner,'' as previously shown.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        A change to the defined restricted area has no affect on any 
    plant operating parameters. Consequently, a change to the defined 
    restricted area will not affect the probability or consequences of 
    an accident occurring.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed revisions to the HBPP TS are administrative in 
    nature. Further, the proposed changes would not result in any 
    physical alteration to any plant system, and there would not be a 
    change in the method by which any safety-related system performs its 
    function.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed revisions to the HBPP TS do not affect the margin 
    of safety of any accident analysis since they do not affect the 
    parameters for any accident analysis, and have no effect on the 
    current operating methodologies or actions which govern plant 
    performance.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Humboldt County Library, 636 F 
    Street, Eureka, California 95501
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas & 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Branch Chief: John H. Austin
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: October 29, 1993
        Description of amendment request: The amendment would revise the 
    Limerick Generating Station, Units 1 and 2, Technical Specifications to 
    eliminate the Main Steam Line Radiation Monitoring System high 
    radiation trip function for initiating 1) an automatic reactor scram 
    and automatic closure of the Main Steam Line Isolation Valves, and 2) 
    automatic closure of the Main Steam Line drain valves, and Main Steam 
    and Reactor Water Sample line valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specification (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS changes involve eliminating the Main Steam Line 
    Radiation Monitoring (MSLRM) system high radiation trip function for 
    initiating an automatic reactor scram and automatic closure of the 
    Main Steam Line Isolation Valves (MSIVs), Main Steam line drain 
    valves, and Main Steam and Reactor Water sample line valves. The 
    proposed TS changes support installation of a plant modification to 
    defeat portions of MSLRM system high radiation trip function logic 
    circuitry in the Reactor Protection System (RPS) and Primary 
    Containment and Reactor Vessel Isolation Control System (PCRVICS). 
    Installation of this modification will not adversely impact the 
    operation of the RPS or PCRVICS with respect to performing its other 
    intended safety functions. The proposed TS changes will not affect 
    the operation of other plant systems or equipment important to 
    safety. The MSLRM system high radiation trip function for the 
    Mechanical Vacuum Pump (MVP) will be retained. The safety assessment 
    and justification for eliminating the MSLRM system high radiation 
    trip function for initiating an automatic reactor scram and 
    automatic closure of the MSIVs [are] based on General Electric's 
    (GE's) Topical Report NEDO-31400A, ``Safety Evaluation for 
    Eliminating the Boiling Water Reactor Main Steam Line Isolation 
    Valve Closure Function and Scram Function of the Main Steam Line 
    Radiation Monitor,'' and the applicability of this report to 
    Limerick Generating Station (LGS), Units 1 and 2. By letter dated 
    May 15, 1991, the NRC approved this topical report and indicated 
    that it was acceptable for licensees to reference this report as the 
    basis for requesting a TS change to eliminate the MSLRM system high 
    radiation trip functions as documented in the report and associated 
    NRC Safety Evaluation Report (SER).
        The safety assessment provided in NEDO-31400A can also be 
    applied to eliminate the MSLRM system high radiation trip function 
    for initiating the automatic closure of the Main Steam line drain 
    valves although this aspect was not explicitly evaluated in NEDO-
    31400A. The flow from these valves ultimately discharges to the main 
    condenser as do the MSIVs and therefore, any radioactive material 
    passing through these valves would be processed in the same fashion 
    as that passing through the MSIVs. The effects of eliminating the 
    MSLRM system high radiation trip function for initiating the closure 
    of the Main Steam and Reactor Water sample line valves is [are] 
    negligible. The sample lines are routed to a sample sink where inlet 
    valves installed on the sample lines are normally closed. 
    Additionally, downstream of the inlet valves are needle valves 
    designed to control and limit sample line flow. The sample sink is 
    enclosed, and air vented from its exhaust hood is passed through 
    filters prior to release to the environment. There is the potential 
    that a minimal amount of radioactive material could be released to 
    the environment if the sample sink inlet and needle valves failed to 
    properly function. This potential release has been evaluated and 
    determined to a small fraction of the dose limit requirements 
    specified in 10 CFR 100.
        The MSLRM system high radiation trip was intended to function in 
    response to a Control Rod Drop Accident (CRDA), a Design Basis 
    Accident previously evaluated. Although the CRDA assumes MSIV 
    closure, no credit was taken for this in the CRDA analysis since it 
    postulates that the radioactive material calculated to be released 
    from the fuel is transported to the main condenser prior to the 
    MSIVs completely closing. Furthermore, the probability of a fuel 
    failure is independent of the operation of the MSLRM system.
        The Steam Jet Air Ejectors (SJAEs) will continue to operate to 
    remove non-condensable gases from the main condenser for processing 
    by the Offgas Treatment system. The Offgas Treatment system will 
    continue to function as designed to reduce offgas radioactivity 
    levels prior to release to the environment. Eliminating the MSLRM 
    system high radiation isolation functions will improve operational 
    flexibility in that the main condenser will be available to aid in 
    decay heat removal. Elimination of the MSLRM system high radiation 
    trip functions in conjunction with proper operation of the Offgas 
    Treatment system will ensure that any radioactive material released 
    to the environment is a small fraction of 10 CFR 100 limits.
        Therefore, the proposed TS changes associated with eliminating 
    the MSLRM system high radiation trip function for initiating an 
    automatic reactor scram and automatic closure of the MSIVs, Main 
    Steam line drain valves, and Main Steam and Reactor Water sample 
    line valves do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes involve eliminating the MSLRM system 
    high radiation trip function for initiating an automatic reactor 
    scram and automatic closure of the MSIVs, Main Steam Line drain 
    valves, and Main Steam and Reactor Water sample line valves. The 
    proposed TS changes will not affect the operation of other plant 
    systems or equipment important to safety. The associated plant 
    modification simply defeats the MSLRM system high radiation trip 
    function logic circuitry in the RPS and PCRVICS. The RPS and PCRVICS 
    will continue to respond in performing its other design intended 
    safety functions. The MSLRM system high radiation trip function for 
    the MVP will be retained. The proposed TS changes do not involve any 
    plant hardware changes that could introduce any new failure modes or 
    effects. The MSLRM system radiation monitors will remain active to 
    initiate Main Control Room (MCR) annunciation alarms. Plant 
    procedures will be in place to implement the appropriate mitigative 
    measures in response to a MSLRM system high radiation alarm signal.
        The SJAEs will continue to operate to remove non-condensable 
    gases from the main condenser for processing by the Offgas Treatment 
    system. The Offgas Treatment system will continue to function as 
    designed to reduce offgas radioactivity levels prior to release to 
    the environment.
        Since the Design Basis Accident analysis (i.e., CRDA) does not 
    credit the MSLRM system high radiation trip function for reducing 
    the radiological consequences of the postulated accident, the 
    proposed TS changes have effectively been evaluated and are included 
    in the existing analysis. That is, the CRDA analysis already assumes 
    that the radioactive material released from the failed fuel is 
    immediately transported to the main condenser prior to the MSIVs 
    completely closing.
        The safety assessment and assumptions documents in GE Topical 
    Report NEDO-31400A provide the basis for eliminating the MSLRM 
    system high radiation trip function for initiating an automatic 
    reactor scram and automatic closure of the MSIVs. The safety 
    assessment provided in NEDO-31400A can also be applied to eliminate 
    the MSLRM system high radiation trip function for initiating the 
    closure of the Main Steam Line drain valves, since any radioactive 
    material passing through these valves would be processed in the same 
    fashion as that passing through the MSIVs. Eliminating the MSLRM 
    system high radiation trip function for initiating the closure of 
    the Main Steam and Reactor Water sample line valves will have a 
    negligible impact. The sample lines are routed to a sample sink 
    where inlet valves installed on the sample lines are normally 
    closed. Downstream of the inlet valves are needle valves designed to 
    control and limit sample line flow. The sample sink is located in 
    the Reactor Enclosure and is enclosed, and air vented from its 
    exhaust hood is passed through filters prior to release to the 
    environment. The Reactor Enclosure ventilation duct radiation 
    monitor samples air from the sample sink hood exhaust, and will 
    isolate the Reactor Enclosure ventilation system if the radiation 
    levels exceed the monitor's setpoint. There is the potential that a 
    minimal amount of radioactive material could be released to the 
    environment through this flowpath if the sample sink inlet and 
    needle valves failed to properly function. This potential release 
    has been evaluated and determined to a small fraction of the dose 
    limit requirements specified in 10CFR100.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The proposed TS changes to eliminate the MSLRM system high 
    radiation trip function for initiating an automatic reactor scram 
    and automatic closure of the MSIVs, Main Steam line drains valves, 
    and Main Steam and Reactor Water sample line valves do not change 
    the conclusion reached in the LGS Updated Final Safety Analysis 
    Report (UFSAR) that the calculated radiological consequences of the 
    bounding Design Basis Accident (i.e., CRDA) will not exceed the dose 
    limit requirements established by 10 CFR 100. The proposed TS 
    changes will improve the overall reliability of the plant when 
    compared to the existing system lineup configuration, since it will 
    reduce the potential of an unnecessary plant transient occurring as 
    a result of an inadvertent MSIV closure.
        A reliability assessment analysis was performed to evaluate the 
    effects of eliminating the MSLRM system high radiation reactor scram 
    function on reactivity control failure frequency and core damage 
    frequency in GE Topical Report NEDO-31400A. This analysis indicated 
    that there is a negligible increase in reactivity control frequency 
    with the elimination of the MSLRM trip function. However, this 
    increase is compensated for by the reduction in transient initiating 
    events (i.e., inadvertent reactor scrams). This reduction in 
    transient initiating events represents a reduction in core damage 
    frequency and thus, results in a net improvement in safety.
        Therefore, the proposed TS changes do not involve a reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Larry E. Nicholson, Acting
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: November 30, 1993
        Description of amendment request: The amendment would extend the 
    surveillance interval of the primary containment drywell-to-suppression 
    chamber bypass leak test from the current 18-month interval as required 
    by Technical Specification (TS) Surveillance Requirement 4.6.2.1.d to a 
    40 +/- 10-month interval. This change would allow the drywell-to-
    suppression chamber bypass test to coincide with the 10 CFR 50, 
    Appendix J, Type A test (i.e., Containment Integrated Leakage Rate Test 
    (CILRT)) interval.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The failure effects that are potentially created by the proposed 
    Technical Specifications (TS) changes have been considered. The 
    accident which is potentially negatively impacted by the proposed TS 
    changes are any Loss of Coolant Accident (LOCA) inside primary 
    containment with or without offsite power available.
        The proposed TS changes increase the surveillance interval of 
    the drywell-to-suppression chamber bypass leak test required by TS 
    Section 4.6.2.1.d, and will require that an additional test be 
    performed on the downcomer vacuum breakers assemblies. The primary 
    containment structure and associated equipment are not considered to 
    be accident initiators, they act to mitigate the consequences of an 
    accident. There are no physical or operational changes being made as 
    a result of these proposed changes. Therefore, the probability of 
    occurrence of an accident previously evaluated is not increased.
        There is a potential increased risk that an increase in the 
    bypass leakage may go undetected for the duration of the proposed 
    extension of the interval between the performance of the drywell-to-
    suppression chamber bypass leak test. However, as discussed below, 
    the increased risk is considered to be negligible due to the design 
    of the diaphragm structure and past test data. Therefore, we have 
    concluded that the probability of bypass leakage exceeding the 
    allowed value is not increased as a result of the proposed TS 
    changes.
        The proposed TS changes will extend the surveillance interval 
    for the drywell-to-suppression chamber bypass leak test from 18 
    months to 40 +/- 10 months. These proposed changes would allow this 
    test to be performed at the same interval as the 10CFR50, Appendix 
    J, Type A test (i.e., Containment Integrated Leakage Rate Test 
    (CILRT)). In addition, the proposed changes will add an additional 
    surveillance requirement to be performed on the vacuum breaker 
    assemblies during refueling outages when the drywell-to-suppression 
    chamber bypass leak test is not required to be performed. The 
    proposed TS changes do not increase the consequences of an accident 
    previously evaluated. This is based on the evaluation summarized 
    below that demonstrates that the overall impact, if any, on the 
    plant containment integrity is negligible. Furthermore, the 
    performance history for the previous LGS bypass leak tests does not 
    indicate any time based failures. The proposed TS changes also 
    include a change to the frequency of testing, if two consecutive 
    tests fail, from once every nine (9) months to once every 24 months 
    in order to coincide with the 24 month refueling cycle. This change 
    has no impact on the consequences of an accident based on 
    maintaining the original requirement to increase the frequency of 
    testing if two consecutive bypass leak tests fail, and maintaining a 
    TS requirement for the NRC to review the schedule for subsequent 
    tests.
        During a LOCA inside containment, potential leak paths between 
    the drywell and suppression chamber airspace could result in 
    excessive containment pressures, since the steam flow into the 
    airspace would bypass the heat sink capabilities of the suppression 
    pool. The containment pressure response to the postulated bypass 
    leakage can be mitigated by manually actuating the suppression 
    chamber sprays. Accordingly, since the sprays are manually actuated, 
    an analysis was performed to show that the operator has sufficient 
    time to initiate the sprays prior to exceeding the containment 
    design pressure. This analysis is described in section 6.2.1.1.5 of 
    the LGS Updated Final Safety Analysis Report (UFSAR). The analysis 
    is based on a small break LOCA inside containment with a 
    differential pressure between the drywell-to-suppression chamber 
    equal to the static pressure due to downcomer submergence. The 
    analysis concludes that the containment design pressure of 55 psig 
    will be reached in over 30 minutes from the onset of a small break 
    LOCA assuming a drywell-to-suppression chamber bypass flow area 
    (i.e., A/square root of k) equal to 7.20 in2 without operator 
    intervention.
        TS Limiting Condition for Operation 3.6.2.1.b conservatively 
    specifies a maximum allowable bypass area of 10 % of the design 
    value of 7.20 in2. This TS limit provides an additional safety 
    factor of 10 above the conservatism taken in the steam bypass 
    analysis (i.e., 0.720 in2). The drywell-to-suppression chamber 
    bypass leak test required by TS Surveillance Requirement 4.6.2.1.d 
    verifies that the actual bypass flow area is less than or equal to 
    the TS limit of 0.720 in2. The bypass leakage test ensures that 
    degradation in the measured bypass area is identified and corrected 
    to ensure containment integrity during LOCA events.
        The potential bypass leakage paths can be divided into two 
    categories as described below.
        1) Leakage pathways other than those associated with the 
    drywell-to-suppression chamber vacuum breaker assemblies such as 
    diaphragm floor penetrations (i.e., downcomer and Safety/Relief 
    Valve (SRV) discharge line penetrations), cracks in the diaphragm 
    floor and/or liner plate, and cracks in the downcomers and SRV 
    discharge lines that pass through the suppression chamber airspace.
        2) The four sets of drywell-to-suppression chamber vacuum 
    breaker assemblies.
        All other potential bypass leakage pathways have at least two 
    isolation valves in the potential leakage path. These valves are 
    high quality leak-tight containment isolation valves that are 
    normally closed and receive an isolation signal to close. All Air 
    Operated Valves (AOVs) in these paths fail closed.
        Several plant design features and the bypass leak test data 
    measured to date confirm that the leakage from other than the vacuum 
    breaker assemblies is negligible and indicates that this leakage 
    will continue to be negligible for the proposed increased duration 
    between tests. All pressure boundary penetrations between the 
    drywell and the suppression chamber are welded except the vacuum 
    breaker valves and the blind flanges closing 10 spare nozzles in the 
    downcomers. All pressure boundary penetrations between the drywell-
    to-suppression chamber have been fabricated, erected, and inspected 
    in accordance with the American Society of Mechanical Engineers 
    (ASME) Code, Section III, Subsection NC, 1971 Edition, with the 
    exception of the tees supporting the vacuum breakers.
        The downcomer and SRV discharge lines penetrate through the 
    diaphragm slab and terminate in the suppression pool. A steel ring 
    plate is welded to the outside of the downcomers. The downcomer/ring 
    plate assemblies are embedded in the diaphragm slab with the top 
    surface of the ring plate flush with the drywell side of the 
    diaphragm slab. All connections are welded to form a continuous 
    steel membrane between the liner plate and downcomer penetrations. 
    The SRV discharge lines are routed through welded flued heads at the 
    diaphragm floor. The flued head design and construction are similar 
    to the downcomer penetrations and also provide a continuous steel 
    barrier. The downcomer and SRV discharge lines are designed and 
    constructed to safety-related requirements. In addition, they are 
    designed for all postulated loading conditions, including seismic, 
    hydrodynamic, pressure, and temperature loads. The conservative 
    design requirements ensure that the SRV discharge and the downcomer 
    lines will not contribute to bypass leakage.
        The diaphragm floor is a reinforced concrete slab approximately 
    3.5 feet thick. The drywell side surface of the diaphragm slab is 
    capped with a 1/4 inch thick carbon steel liner plate. The liner 
    plate and diaphragm slab provide a barrier against the potential for 
    bypass leakage through the diaphragm floor. The structural integrity 
    of the diaphragm floor and penetrations was demonstrated during the 
    pre-operational test program. The drywell was pressurized to a 
    drywell-to-suppression chamber differential pressure of above 30 
    psid, which envelopes the maximum drywell-to-suppression chamber 
    differential pressure postulated to occur during LOCA conditions.
        There have been six Unit 1 and three Unit 2 bypass leak tests 
    performed in accordance with TS Surveillance Requirement 4.6.2.1.d. 
    These tests were conducted at a drywell-to-suppression chamber 
    differential pressure of at least 4.0 psid. The measured leakage 
    area includes leakage from both the vacuum breakers and sources 
    other than vacuum breakers.
        In all cases, the measured leakage is significantly less than 
    the TS and design values. The maximum measured leakage areas are 
    0.0400 in2 and 0.0111 in2 for Unit 1 and Unit 2, 
    respectively; or 5.56% and 1.55 %, respectively, of the TS limit. 
    The average values are 0.0180 in2 for Unit 1 and 0.0107 
    in2 for Unit 2; or 2.5% and 1.49%, respectively, of the TS 
    limit of 0.720 in2. The minimum measured leakage areas are 0.0 
    in2 and 0.0100 in2 for Unit 1 and Unit 2, respectively, or 
    0% and 1.3 %, respectively, of the TS limit. Clearly, the test data 
    confirm that the bypass leakage measured to date at LGS has been 
    negligible.
        In addition, we have obtained bypass leakage data from the 
    Pennsylvania Power and Light Company, Susquehanna Steam Electric 
    Station (SSES), Units 1 and 2, which also has Mark II containments 
    with the Anderson Greenwood vacuum breakers (i.e., the same 
    manufacturer as the vacuum breakers installed in the LGS, Unit 1 and 
    Unit 2 containments) and therefore the data is applicable to LGS. 
    The maximum bypass leakage area for the SSES Unit 1 containment was 
    0.037 in2, and 0.009 in2 for the SSES Unit 2 containment, 
    or 4.81% and 1.17%, respectively, of the SSES TS limit. Approval for 
    a similar TS change for SSES, Units 1 and 2 was issued by the NRC by 
    letter dated August 11, 1993.
        The remaining and most likely source of potential bypass leakage 
    is the four sets of drywell-to-suppression chamber vacuum breakers. 
    Each set consists of two vacuum breakers in series, flange mounted 
    to a tee off the downcomers in the suppression chamber airspace. The 
    drywell-to-suppression chamber bypass leak test is currently 
    required by TS Surveillance requirement 4.6.2.1.d to be completed 
    during each refueling outage and the results are used to verify that 
    the total bypass area, including that due to the vacuum breakers, 
    meets the TS limit. If maintenance has been performed on the vacuum 
    breakers, this test also serves as a post-maintenance vacuum 
    breakers leakage area test.
        The proposed TS changes decrease the frequency of the drywell-
    to-suppression chamber bypass leak test. The drywell-to-suppression 
    chamber bypass leak test data obtained following vacuum breakers 
    maintenance cannot be utilized to determine vacuum breakers leakage 
    reliability over the duration of the proposed test interval 
    extension. To address this concern and collect additional vacuum 
    breakers leakage data, the proposed TS changes include an additional 
    requirement to perform a vacuum breaker leakage test as described 
    below.
        The leakage test will be conducted on each set of vacuum 
    breakers (i.e., four vacuum breakers sets per unit) during each 
    refueling outage when the drywell-to-suppression chamber bypass leak 
    test would not be required to be performed. If maintenance is 
    performed on the vacuum breaker assemblies, this additional test 
    will be performed post-maintenance to verify that the leakage is 
    acceptable. This test will be conducted at a drywell-to-suppression 
    chamber differential pressure of 4.0 psid (i.e., the same as 
    differential pressure required for the drywell-to-suppression 
    chamber bypass leak test) by either pressurizing the drywell side of 
    the vacuum breakers or inducing a vacuum on the suppression chamber 
    side of the vacuum breakers. The acceptance criteria for the vacuum 
    breaker leakage tests will be as follows. The total vacuum breaker 
    leakage areas for all four sets of vacuum breakers will be less than 
    or equal to 24% of the TS limit (i.e., 0.24 x 0.720 in2 = 0.173 
    in2). This proposed acceptable vacuum breaker leakage area 
    provides a 76% margin to the TS limit to account for the leakage 
    paths other than the vacuum breakers. As described above, previous 
    bypass leakage testing measured a maximum bypass leakage area of 
    5.56% of the TS limit. The 76% margin is sufficiently large to 
    accommodate the other expected leakage sources. In addition, each 
    set of vacuum breakers will be limited to a leakage area twice the 
    assumed leakage from a single vacuum breaker set, assuming the 
    leakage area is evenly distributed among the four sets of vacuum 
    breakers (i.e., four sets equate to 24% of the TS Limit where each 
    set is 6% and twice this total is 12% of the TS Limit). This allows 
    a leakage of less than or equal to 0.0865 in2 (i.e., (0.173 
    in2 divided by 4 sets of vacuum breakers) x (a factor of 2 
    times the acceptable total) = 0.0865 in2) for an individual set 
    of vacuum breakers. This criterion is stipulated to identify 
    individual sets of vacuum breakers with higher leakage area.
        The drywell-to-suppression chamber bypass leak test data 
    obtained during previous testing at LGS demonstrates conformance by 
    a large margin compared to the TS and design leakage requirements. 
    The test data indicates that there is negligible risk that the 
    bypass leakage will change adversely in future years. Furthermore, 
    the proposed test frequency is judged to be acceptable based on the 
    risk of the leakage sources other than the vacuum breakers being 
    essentially equivalent to that of the rest of the primary 
    containment structure, which is leak tested (i.e., CILRT) every 40 
    +/- 10 months as required by TS Surveillance Requirement 4.6.1.2.a. 
    A bypass leak test will be developed and conducted to verify 
    acceptable vacuum breaker bypass leakage areas for those outages 
    when the bypass leak test will not be required to be performed. The 
    proposed vacuum breaker leakage test with stringent acceptance 
    criteria, combined with other negligible leakage areas, provide an 
    acceptable level of assurance that the bypass leakage can be 
    measured and an adverse condition can be detected and corrected such 
    that the existing level of confidence that the primary containment 
    will function as required during a LOCA is maintained.
        Therefore, the proposed TS changes will not involve an increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes involve the drywell-to-suppression 
    chamber bypass leak test frequency. There are no physical or 
    operational changes as a result of these proposed changes. These 
    proposed changes include the requirement to perform an additional 
    surveillance test on the vacuum breaker assemblies, applying a 
    differential pressure of 4.0 psid which is the same differential 
    pressure as currently required by TS for the drywell-to-suppression 
    chamber bypass leak test. This required test will ensure that 
    acceptable vacuum breaker leakage is maintained during those 
    intervals when the drywell-to-suppression chamber bypass leak test 
    is not required to be performed. Furthermore, the affected structure 
    (i.e., primary containment) acts as an accident mitigator and not as 
    an accident initiator. Accordingly, the possibility of a different 
    type of malfunction of equipment or the possibility of an accident 
    of a different type is not introduced.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The drywell-to-suppression chamber bypass leak test data 
    obtained during previous testing at LGS demonstrates conformance by 
    a large margin to the TS and design leakage requirements. The test 
    data indicate that there is negligible risk that the bypass leakage 
    will change adversely in future years. Furthermore, the proposed 
    test frequency is judged to be acceptable based on the risk of 
    sources of leakage other than the vacuum breakers being essentially 
    equivalent to that of the rest of the primary containment structure, 
    which is tested every 40 +/- 10 months. A bypass leak test will be 
    developed and conducted to verify acceptable vacuum breaker bypass 
    leakage areas for those outages when the bypass leak test will not 
    be required to be performed. The proposed vacuum breaker leakage 
    test with stringent acceptance criteria, combined with the other 
    negligible potential leakage areas, provide an acceptable level of 
    assurance that the bypass leakage can be measured and an adverse 
    condition can be detected and corrected such that the existing 
    levels of confidence that the primary containment will function as 
    required during a LOCA is maintained.
        Therefore, the consequences of an accident are not impacted by 
    this change and containment integrity during a LOCA will be 
    maintained.
        Therefore, the proposed TS changes do not involve a reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Larry E. Nicholson, Acting
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company, Delmarva Power and Light Company, and Atlantic City 
    Electric Company, Dockets Nos. 50-277 and 50-278, Peach Bottom 
    Atomic Power Station, Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 17, 1993
        Description of amendment request: The proposed Technical 
    Specification (TS) changes to Surveillance Requirements would eliminate 
    unnecessary emergency diesel generator (EDG) testing when a diesel 
    generator or an offsite power source becomes inoperable. The proposed 
    change would reduce the stresses on the diesel generators caused by 
    unnecessary testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because implementation of the proposed TS change, which 
    would delete the requirement to demonstrate the operability of an 
    otherwise operable EDG once the potential for a common cause failure 
    has been dismissed, does not affect the design or performance 
    characteristics of an EDG. Similarly, deleting the requirement to 
    demonstrate the operability of EDGs when an offsite power source is 
    inoperable does not affect the design or performance characteristics 
    of an EDG. Therefore, the EDGs will maintain their ability to 
    perform their design function. The EDGs are not assumed to be an 
    initiator of any analyzed event. The role of the EDGs is the 
    mitigation of accident consequences. Therefore, this proposed TS 
    change does not increase the probability of an accident previously 
    evaluated.
        The consequences of an accident previously evaluated could be 
    affected by the proposed TS change. As described above, 
    implementation of the proposed change will result in the EDGs 
    maintaining their ability to perform their design function. 
    Excessive testing of EDGs can cause reduced reliability. Precluding 
    unnecessary testing of operable EDGs will improve EDG reliability 
    and thereby have an overall positive affect on plant safety. 
    Therefore, this proposed TS change does not increase the 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because implementation of the proposed TS change will not involve 
    physical changes to plant systems, structures, or components (SSC). 
    The design or performance characteristics of the EDG will not be 
    affected by the proposed change. The proposed change does not 
    introduce any new modes of plant operation or make any changes to 
    system setpoints which would initiate a new or different kind of 
    accident. Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated is not created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety because the proposed TS change does not affect 
    the design or performance of any EDG. The change will increase EDG 
    reliability by reducing the stresses on the EDG from unnecessary 
    testing. This will result in an overall increase in plant safety. 
    Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Charles L. Miller
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company, Delmarva Power and Light Company, and Atlantic City 
    Electric Company, Dockets Nos. 50-277 and 50-278, Peach Bottom 
    Atomic Power Station, Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 19, 1993
        Description of amendment request: The proposed change would 
    eliminate the listing of specific position titles for the Plant 
    Operations Review Committee (PORC) composition in favor of allowing the 
    Plant Manager to appoint PORC members. This would eliminate the need to 
    change the Technical Specifications (TSs) in the future whenever a 
    position title is changed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because the proposed TS change is administrative in 
    nature. The PORC member titles will be removed from the TS to 
    facilitate not requiring that a TS change be submitted for NRC 
    approval when position titles change. PORC member qualifications 
    will continue to be consistent with those required for the Facility 
    Staff and meet or exceed Sections 4.2, 4.4, or 4.6 of ANSI N18.1-
    1971. The proposed change ensures that PORC will continue to be 
    comprised of personnel involved in daily plant activities who are 
    experienced individuals with varied expertise. By maintaining the 
    qualification requirements for members of PORC who represent various 
    areas of expertise, PORC will continue to fulfill its requirements 
    specified in TS Section 6.5.1.6. The proposed change does not 
    involve any physical changes to plant systems, structures, or 
    components (SSC), or the manner in which these SSC are operated, 
    maintained, modified, tested, or inspected. Therefore, the proposed 
    TS change does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because implementation of the proposed TS change will not involve 
    physical changes to plant SSC or the manner in which these SSC are 
    operated, maintained, modified, tested or inspected. The proposed 
    change does not introduce any new modes of plant operation or make 
    any changes to system setpoints which would initiate a new or 
    different kind of accident. Therefore, the possibility of a new or 
    different kind of accident from any accident previously evaluated is 
    not created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety because the proposed TS change is 
    administrative in nature by providing internal flexibility in 
    changing organizational titles and does not reduce the PORC function 
    or responsibilities. PORC will continue to be filled by 
    appropriately qualified personnel who have a variety of expertise. 
    The change does not affect the plant material condition, operation, 
    or accident analyses. Therefore, the proposed change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Charles L. Miller
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama
    
        Date of amendments request: November 24, 1993
        Description of amendments request: The proposed changes to the 
    Technical Specification will relocate the reactor trip system and 
    engineered safety feature actuation system response time limits from 
    the TS to the Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The proposed changes are administrative in nature and do not involve 
    any change to the configuration or method of operation of any plant 
    equipment used to mitigate the consequences of an accident. Also, 
    the proposed changes do not alter the conditions or assumptions in 
    any of the FSAR accident analyses. Since the FSAR accident analyses 
    remain bounding, the radiological consequences previously evaluated 
    are not adversely affected by the proposed changes. Therefore, the 
    proposed changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The proposed changes are administrative in nature and do 
    not involve any change to the configuration or method of operation 
    of any plant equipment used to mitigate the consequences of an 
    accident.Accordingly, no new failure modes have been defined for any 
    plant system or component important to safety nor has any new 
    limiting failure been identified as a result of the proposed 
    changes. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety. The proposed changes are administrative in 
    nature and will continue to ensure that the response times for the 
    RTS and ESFAS instrumentation do not exceed the limits assumed in 
    the accident analyses. As a result of the proposed changes, response 
    time limits for the RTS and ESFAS will be administratively 
    controlled in accordance with the provisions of 10 CFR 50.59, thus 
    eliminating an unnecessary burden of governmental regulation without 
    reducing protection for public health and safety. Therefore, the 
    proposed changes do not involve a significant reduction in a margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Attorney for licensee: James H. Miller, III, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: S. Singh Bajwa
    
    Tennessee Valley Authority (TVA), Docket Nos. 50-259, 50-260 and 
    50-296, Browns Ferry Nuclear Plant (BFN), Units 1, 2, and 3, 
    Limestone County, Alabama
    
        Date of amendment request: September 30, 1993 (TS 337)
        Description of amendment request: The proposed amendments provide 
    an administrative vehicle for modifying a condition of the facility 
    operating license for each of the BFN units. The condition requires the 
    licensee to implement and maintain in effect all provisions of the 
    ``Fire Protection Program (FPP)'' and lists the U.S. Nuclear Regulatory 
    Commission (NRC) staff safety evaluations (SE) approving the FPP. If 
    the staff approves of a revision currently under review to an element 
    of the FPP, the ``Appendix R Safe Shutdown Program (SSP)'', the 
    proposed amendments would add the staff SE documenting approval of the 
    revised SSP to the above listing of SEs in each facility operating 
    license. The current SSP is directed toward the safe shutdown of only 
    one operating plant (Unit 2). The revised SSP would be directed toward 
    the safe shutdown of two operating plants (Units 2 and 3).
        Additionally, the proposed amendments add the definition of the SSP 
    to Section 1.0 of the Unit 3 Technical Specifications (TS).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        This proposed change is administrative in nature. The proposed 
    change is being made to revise the license condition to reflect a 
    combined Unit 2 and 3 Appendix R Safe Shutdown Program following NRC 
    approval. Compliance with the applicable Appendix R requirements is 
    ensured through implementation of the Fire Protection Program and 
    the Appendix R Safe Shutdown Program. The change does not affect any 
    design bases accident or the ability of any safe shutdown equipment 
    to perform its function. Also, there are no physical modifications 
    required to implement this TS change. Therefore, these proposed 
    administrative changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change is administrative in nature. The proposed 
    change is being made to revise the license condition to reflect a 
    combined Unit 2 and 3 Safe Shutdown Program following NRC approval. 
    Compliance with the applicable Appendix R requirements is ensured 
    through implementation of the Fire Protection Program and Appendix R 
    Safe Shutdown Program. This change does not affect any design basis 
    accident or the ability of any safe shutdown equipment to perform 
    its function. Also, there are no physical modifications required to 
    implement this TS change. Therefore, these proposed administrative 
    changes do not create the possibility of a new or different kind of 
    accident from an accident previously evaluated.
        3. This change does not involve a significant reduction in the 
    margin of safety.
        The proposed changes are administrative in nature. Compliance 
    with the applicable Appendix R requirements is ensured through the 
    implementation of the Fire Protection Program and Appendix R Safe 
    Shutdown Program. The proposed change does not affect any design 
    basis accident and does not reduce or adversely affect the 
    capability to achieve and maintain safe shutdown in the event of a 
    fire. Furthermore, no reductions to the requirements for equipment 
    operability, surveillance requirements or setpoints are being made 
    which could result in reduction in the margin of safety. Therefore, 
    these proposed administrative changes will not result in a reduction 
    in the margin of safety.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Mr. Frederick J. Hebdon
    
    Tennessee Valley Authority (TVA), Docket Nos. 50-259, 50-260 and 
    50-296, Browns Ferry Nuclear Plant (BFN), Units 1, 2, and 3, 
    Limestone County, Alabama
    
        Date of amendment request: October 12, 1993 (TS 320)
        Description of amendment request: The proposed amendment would 
    delete reference in the BFN Unit 3 Technical Specifications (TS) to the 
    Reactor Water Cleanup (RWCU) system floor drain high temperature 
    switches and the RWCU system space high temperature switches. The 
    piping configuration for the Unit 3 RWCU system has been modified, and 
    the licensee contends that its revised High Energy Line Break (HELB) 
    analysis has demonstrated that these switches are no longer required. 
    Instead, to initiate RWCU system isolation, the HELB analysis has 
    indicated the need for temperature switches in the main steam vault, 
    the heat exchanger room, and the RWCU pipe trench. The proposed 
    amendment therefore would add temperature switches to the Unit 3 TS for 
    these areas and modify the TS Bases section accordingly. The proposed 
    amendment also adds clarifying remarks to Tables 3.2.A and 3.2.B of the 
    TS for each of the BFN units. The proposed remarks list the actuation 
    signals for the various primary containment valve group isolations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        An analysis of HELBs in the Unit 3 reactor building identified 
    certain RWCU pipe breaks which could not be automatically detected 
    and isolated in a reasonable time frame. To resolve this issue, a 
    design change is being performed to remove from service the existing 
    non-environmentally qualified temperature switches used to detect 
    RWCU line breaks and replace them with environmentally qualified 
    RTDs [resistance temperature detectors] and IEEE [Institute of 
    Electrical and Electronics Engineers] Class 1E qualified ATUs 
    [analog trip units] located to detect and isolate the critical RWCU 
    pipe breaks. This TS amendment adds the new ATUs [sic] function to 
    Tables 3.2.A and 4.2.A. Note 14 is deleted from Table 3.2.A since it 
    only applies to the temperature switches being removed from the 
    table.
        The safety function of the RTD/ATU temperature loops is to 
    provide an isolation signal to close the RWCU suction line isolation 
    valves (FCV-69-001 and FCV-69-002) and RWCU return line valve (FCV-
    69-012) on a high area temperature. This ensures RWCU pipe breaks 
    are isolated. No other RWCU safety functions are affected by the 
    change.
        The new RTD/ATU temperature loops were chosen to decrease the 
    time required to initiate closure of the RWCU valves. This improves 
    the detection/isolation of RWCU breaks and helps to limit the 
    reactor coolant lost, helps ensure core cooling, and helps ensure 
    that environmental conditions inside the reactor building are 
    maintained within the required limits.
        Components added by this change are qualified for the 
    environment in which they will operate. This ensures that the system 
    will perform its function in a post accident environment. No 
    additional paths for the release of radiation or contamination are 
    created. The failure modes of the RTDs and ATUs are such that any 
    single failure will result in a gross failure alarm and/or a channel 
    trip. Because of the redundancy, separations, and logic designed 
    into the system, a single failure of any part of the system will not 
    prevent isolation of the primary containment isolation valves and 
    spurious operation is minimized. The RTDs will be located and the 
    instrument setpoints will be set to preclude spurious trips due to 
    ambient temperatures including localized hot areas while assuring a 
    timely trip due to a pipe break. Therefore, the proposed amendment 
    does not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        This change is being made to improve the RWCU leak detection/
    isolation function of the RWCU Primary Containment Isolation System 
    (PCIS). The PCIS will perform its intended safety function in the 
    same manner as the previous installation. There is no affect [sic] 
    on the function or operation of any other plant system.
        Failure of the RTD/ATU temperature loops would be no different 
    than failure of existing temperature switches. Since environmental 
    qualification requirements, divisional separation, single failure 
    requirements and one-out-of-two taken twice logic requirements are 
    maintained, the possibility of a RWCU isolation failure on a RWCU 
    line break or of a spurious isolation is no more likely after the 
    change than before.
        In the existing design, logic relays are powered from RPS Bus A 
    or B. The new design also uses RPS Bus A or B to feed the ATUs. 
    Therefore, the consequence of a power failure is unchanged from the 
    present design. The seismic qualification and proper circuit 
    coordination of the installation is maintained. The system functions 
    and operates in the same manner as previously evaluated in the 
    Safety Analysis Report. No new system interactions other than 
    additional RTDs located in the main steam valve vault to input into 
    the PCIS logic for isolation of the RWCU have been introduced by 
    this activity. Therefore, the proposed amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The margin of safety will be enhanced by installing instruments 
    that provide quicker response to a temperature rise indicative of a 
    pipe break. Calculations have been performed to determine the 
    analytical limits for the RTD/ATU temperature loops in each of the 
    monitored areas and to determine the setpoints for the ATUs in each 
    area. The setpoints are set above the maximum expected room 
    temperatures to avoid spurious actuations due to ambient conditions 
    and below the analytical limits to ensure timely detection of a pipe 
    break. This type of design utilizing ATUs has been analyzed by the 
    NRC [U.S. Nuclear Regulatory Commission staff] (NEDO-21617, Analog 
    Transmitter/Trip Unit System for Engineered Safeguard Sensor Trip 
    Input) and has been found to be generically acceptable at BWR 
    facilities. Therefore, the proposed amendment does not involve a 
    significant reduction in any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Mr. Frederick J. Hebdon
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: December 10, 1993
        Description of amendment request: The proposed change would change 
    the Technical Specifications (TS) for the North Anna Power Station, 
    Units No. 1 and No. 2 (NA-1&2).
        Specifically, the proposed changes would modify the surveillance 
    frequency of the Auxiliary Feedwater System pumps from monthly to 
    quarterly in accordance with the guidance provided in Generic Letter 
    93-05, ``Line-Item Technical Specifications Improvements to Reduce 
    Surveillance Requirements for Testing During Power Operation,'' dated 
    September 27, 1993.
        The NRC has completed a comprehensive examination of surveillance 
    requirements in TS that require testing at power. The evaluation is 
    documented in NUREG-1366, ``Improvements to Technical Specification 
    Surveillance Requirements,'' dated December 1992. The NRC staff found, 
    that while the majority of testing at power is important, safety can be 
    improved, equipment degradation decreased, and an unnecessary burden on 
    personnel resources eliminated by reducing the amount of testing at 
    power that is required by TS. Based on the results of the evaluations 
    documented in NUREG 1366, the NRC issued Generic Letter 93-05.
        The Auxiliary Feedwater System supplies water to the steam 
    generators to remove decay heat from the Reactor Coolant System. To 
    ensure operability of the Auxiliary Feedwater System, the pumps are 
    currently tested on a monthly basis as required by the TS. Consistent 
    with Generic Letter 93-05, Item 9.1 and NUREG-1366, the licensee is 
    requesting a change to the surveillance testing frequency for the 
    Auxiliary Feedwater Pumps from monthly to quarterly on a staggered test 
    basis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of North Anna Power Station in 
    accordance with the proposed Technical Specifications changes will 
    not:
        1. Involve a significant increase in the probability of 
    occurrence or consequences of an accident previously evaluated.
        Changing the surveillance test frequencies of the Auxiliary 
    Feedwater System pumps does not significantly affect the probability 
    of occurrence or consequences of any previously evaluated accidents. 
    Quarterly testing of the pumps on a staggered basis will continue to 
    assure that the Auxiliary Feedwater System will be capable of 
    performing its intended functions. Therefore, the change in 
    frequency of testing the Auxiliary Feedwater System pumps does not 
    affect the probability or consequences of any previously analyzed 
    accident.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        Changing the surveillance test frequency of the Auxiliary 
    Feedwater System pumps does not involve any physical modification of 
    the plant or result in a change in a method of operation. Quarterly 
    testing of the Auxiliary Feedwater System pumps on a staggered basis 
    will continue to assure that the Auxiliary Feedwater System will be 
    capable of performing its intended function. Therefore, a new or 
    different type of accident is not made possible.
        3. Involve a significant reduction in a margin of safety.
        Changing the surveillance test frequency of the Auxiliary 
    Feedwater System pumps does not affect any safety limits or limiting 
    safety system settings. System operating parameters are unaffected. 
    The availability of equipment required to mitigate or assess the 
    consequence of an accident is not reduced. Quarterly testing of the 
    Auxiliary Feedwater System pumps on a staggered basis will continue 
    to assure that the Auxiliary Feedwater System will be capable of 
    performing its intended functions. Safety margins are, therefore, 
    not decreased.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Herbert N. Berkow
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: October 5, 1993
        Brief description of amendment: The proposed change to the 
    Technical Specifications would revise the wording of liquid release 
    rate limit and its associated bases, and relocate the old 10 CFR 20.106 
    requirements to the new 10 CFR 20.1302 to be consistent with the 
    revised terminology of 10 CFR Part 20. The new wording will retain the 
    same overall level of effluent control required to meet the design 
    objectives of Appendix I to 10 CFR Part 50.
        Date of issuance: December 14, 1993
        Effective date: December 14, 1993
        Amendment No.: 40
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59746) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 14, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of application for amendments: August 5, 1992
        Brief description of amendments: The amendment revises the 
    Braidwood Station, Units 1 and 2, Technical Specifications (TS) 
    regarding Engineered Safety Features Actuation System (ESFAS) 
    instrumentation. The ESFAS, Functional Units, Analog Channel 
    Operational Test interval is changed from monthly to quarterly. 
    Eighteen changes to the Reactor Trip System (RTS) are also included in 
    this TS change.
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993
        Amendment Nos.: 44 and 44
        Facility Operating License Nos. NPF-72 and NPF-77. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 28, 1992 (57 FR 
    48816) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 16, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Wilmington Township Public 
    Library, 201 S. Kankakee Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: October 29, 1993
        Brief description of amendments: The amendments revise Table 3.6.3-
    1, ``Primary Containment Isolation Valves,'' of the LaSalle Technical 
    Specifications for Units 1 and 2 by adding a new category of valves to 
    these tables. There are a total of eight new valves added in each 
    table, consisting of two check valves in each of four backfill lines. 
    The backfill lines were added in response to NRC Bulletin 93-03, 
    ``Resolution of Issues Related to Reactor Vessel Water Level 
    Instrumentation in BWRs,'' dated May 28, 1993.
        Date of issuance: December 10, 1993
        Effective date: December 10, 1993
        Amendment Nos.: 92 and 76
        Facility Operating License Nos. NPF-11 and NPF-18. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1993 (58 FR 
    59493). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 10, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: November 25, 1992, as 
    supplemented by letter dated February 5, 1993.
        Brief description of amendment: The amendment revises surveillance 
    intervals for Process Radiation Monitors, Area Radiation Monitors, the 
    Main Steam Line Radiation Monitors, the Auxiliary Feedwater System 
    Initiating Logic, the Main Steam Safety Valves Setpoints, and the Toxic 
    Gas Detection System Monitors to accommodate a 24-month refueling 
    cycle. These revisions are being made in accordance with the guidance 
    provided by Generic Letter 91-04, ``Changes in Technical Specification 
    Surveillance Intervals to Accommodate a 24-Month Fuel Cycle.''
        Date of issuance: December 16, 1993
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 166
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 25, 1993 (58 FR 
    16219) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 16, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: October 5, 1993, as 
    supplemented November 15 and 22, 1993
        Brief description of amendments: The amendments revise the 
    Technical Specifications to reflect the appropriate operability 
    requirements for cold leg accumulator water volume and surveillance 
    requirements values for the centrifugal changing pumps, safety 
    injection pumps, and residual heat removal pumps to prevent possible 
    runout conditions during a loss of coolant accident event.
        Date of issuance: December 15, 1993
        Effective date: December 15, 1993
        Amendment Nos.: 110 and 104
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 27, 1993 (58 FR 
    57848) The November 15 and 22, 1993, letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 15, 1993. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: October 5 and 14, 1993, as 
    supplemented November 15 and December 14, 1993
        Brief description of amendments: The amendments revise the 
    Technical Specifications to allow the implementation of interim steam 
    generator tube plugging criteria for the tube support plate elevations.
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993
        Amendment Nos.: 111 and 105
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 27, 1993 (58 FR 
    57849) The November 15 and December 14, 1993, letters provided 
    clarifying information and revisions to the coolant specific activity 
    that did not change the scope of the original application and did not 
    change the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 16, 1993. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: September 7, 1993
        Brief description of amendments: The amendments revise the 
    Technical Specification to (a) reduce the slope of the axial power 
    imbalance penalty in the overtemperature-delta temperature reactor 
    protection system trip setpoint equation, and (b) increase the boron 
    concentration limits in the cold leg accumulators, the refueling water 
    storage tank, the reactor coolant system, and refueling canal during 
    MODE 6 conditions. These changes reflect the reloading of Unit 1 with 
    Mark BW fuel for Cycle 8 including an increase in cycle length from 350 
    effective full power days (EFPD) to 390 EFPD.
        Date of issuance: December 17, 1993
        Effective date: December 17, 1993
        Amendment Nos.: 112 and 106
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 27, 1993 (58 FR 
    57847) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 17, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: October 25, 1993, as 
    supplemented December 3 and 6, 1993
        Brief description of amendments: The amendments revise the 
    Technical Specifications (TS) Figure 2.1-1, certain TS Table 2.2-1 
    factors in the equation for the OVERTEMPERATURE delta T and OVERPOWER 
    delta T setpoints, and Figure 3.2-1 to reflect a reduction in the 
    required minimum measured reactor coolant system (RCS) flow rate from 
    385,000 gallons per minute (gpm) to 382,000 gpm for Unit 1. Catawba 
    Unit 2 values are unchanged and, accordingly, certain TS pages were 
    modified to retain the current TS values in effect for Unit 2.
        The need for these changes is attributed to the effects of steam 
    generator tube plugging and to a hot leg temperature streaming 
    phenomenon. The application also proposed to revise the text of TS 
    2.1.1 and the definition for TS Figure 2.1-1. These changes are not 
    related to the changes in RCS flow rate. The staff is continuing to 
    review these proposed changes and, accordingly, they are not dealt with 
    in this amendment.
        Date of issuance: December 17, 1993
        Effective date: Effective within 30 days of its date of issuance.
        Amendment Nos.: 113 and 107
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59747) The December 3 and 6, 1993, letters provided clarifying 
    information that did not change the scope of the October 25, 1993, 
    application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 17, 1993. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company, Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: May 20, 1993
        Brief description of amendment: The amendment removed unnecessary 
    operability requirements for the Intermediate Range Monitors (IRMs) and 
    the Average Power Range Monitors (APRMs) during plant shutdown 
    operations.
        Date of issuance: December 13, 1993
        Effective date: December 13, 1993
        Amendment No: 109
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34077) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 13, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, Post Office Box 1406, S. Commerce at Washington, Natchez, 
    Mississippi 39120.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: July 23, 1993
        Brief description of amendments: The amendments are necessary to 
    implement new Standards for Protection Against Radiation (10 CFR Part 
    20).
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993
        Amendment Nos.: 125, 63
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46234) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 16, 1993. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: October 8, 1993
        Brief description of amendment: The amendment deletes portions of 
    the Oyster Creek Nuclear Generating Station Radiological Effluent 
    Technical Specifications and relocates them to controlled programs in 
    accordance with the guidance contained in NRC Generic Letter 89-01, 
    dated January 31, 1989.
        Date of issuance: December 13, 1993
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 166
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59749) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated December 13, 1993. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, New Jersey 
    08753.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: October 18, 1993
        Brief description of amendment: The amendment revises the Technical 
    Specifications to delete requirements to demonstrate by testing, that a 
    redundant system/component is operable when a system/component is 
    declared inoperable. In lieu of testing the redundant system/component 
    to demonstrate its operability the Technical Specifications are being 
    revised to require an administrative check of plant records to verify 
    operability of the redundant system/component. Confirming changes are 
    made to Definition 1.1 ``Operable-Operability.''
        Date of issuance: December 21, 1993
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 167
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59749) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 21, 1993. No 
    significant hazards consideration comments received: Yes. Comments were 
    provided by letter dated December 10, 1993, from the State of New 
    Jersey, Department of Environmental Protection and Energy, Division of 
    Environmental Safety, Health and Analytical Programs. The comments and 
    the NRC staff's response are addressed in the Commission's Safety 
    Evaluation dated December 21, 1993.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, New Jersey 
    08753
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: September 20, 1993, as 
    supplemented on October 1, 1993.
        Brief description of amendment: The amendment revises the plant 
    Technical Specifications to reflect a partial GPU Nuclear 
    reorganization to become effective when Three Mile Island, Unit 2 (TMI-
    2), enters the Post-Defueling Monitored Storage (PDMS) mode. This 
    reorganization includes deleting TMI-2 as a Division and incorporating 
    those functions and responsibilities required to maintain the PDMS 
    condition and requirements into the current TMI-1 Division. The TMI-1 
    Division will be renamed the TMI Division.
        Date of issuance: December 13, 1993
        Effective date: No specific date has been specified by the staff 
    for the effectiveness of this amendment. The amendment will become 
    fully effective at such time as the Vice President - TMI has been 
    delegated the full responsibility of the overall safe operation of both 
    TMI-1 and TMI-2.
        Amendment No.: 179
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 13, 1993 (58 FR 
    52987). The October 1, 1993, submittal provided clarifying and 
    corrected TS pages which did not change the initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of this amendment is contained in a Safety 
    Evaluation dated December 13, 1993. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: August 9, 1993
        Brief description of amendment: The amendment revises the plant 
    Technical Specifications to be consistent with a major revision to 10 
    CFR Part 20 that is to be implemented by January 1, 1994.
        Date of issuance: December 21, 1993
        Effective date: As of the date of issuance to be implemented on 
    January 1, 1994.
        Amendment No.: 180
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59751). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 21, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: August 24, 1993.
        Brief description of amendment: The amendment revises the plant 
    Technical Specifications to adopt the Standard Technical Specification 
    (STS) provision that allows a period up to 24 hours to complete a 
    surveillance requirement upon the discovery that the surveillance has 
    been missed.
        Date of issuance: December 22, 1993
        Effective date: As of its date of issuance, to be implemented 
    within 30 days of issuance.
        Amendment No.: 181
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59751). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 22, 1993. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Gulf States Utilities Company and Cajun Electric Power Cooperative, 
    Docket No. 50-458, River Bend Station, Unit 1, West Feliciana 
    Parish, Louisiana
    
        Date of amendment request: January 13, 1993, as supplemented by 
    letter dated October 18, 1993.
        Brief description of amendment: The amendment revises the River 
    Bend, Unit 1 operating license to reflect a change in ownership of Gulf 
    States Utilities (GSU). GSU, which owns a 70 percent undivided interest 
    in the River Bend Station, will become a wholly-owned subsidiary 
    company of Entergy Corporation.
        Date of issuance: December 16, 1993
        Effective date: December 6, 1993, to be implemented within 180 days 
    of issuance.
        Amendment No.: Amendment No. 69
        Facility Operating License No. NPF-47: The amendment revised the 
    license.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36435) The October 18, 1993, supplemental letter provided additional 
    clarifying information and did not change the initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    December 16, 1993. No significant hazards consideration comments 
    received: Yes. Comments and a request for hearing were received from 
    Cajun Electric Power Cooperative of Baton Rouge, Louisiana.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: January 13, 1993, as supplemented by 
    letter dated June 29, 1993.
        Brief description of amendment: The amendment revises the River 
    Bend Station, Unit 1 operating license to include as a licensee, 
    Entergy Operations, Inc. (EOI), and to authorize EOI to use and operate 
    River Bend and to possess and use related licensed nuclear materials.
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993 to be implemented within 180 days 
    of issuance.
        Amendment No.: 70
        Facility Operating License No. NPF-47: The amendment revised the 
    license.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36436) The June 29, 1993, supplemental letter provided additional 
    clarifying information and did not change the initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    December 16, 1993. No significant hazards consideration comments 
    received: Yes. Comments and a request for hearing were received from 
    Cajun Electric Power Cooperative of Baton Rouge, Louisiana.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: June 18, 1993
        Brief description of amendment: The proposed changes to Technical 
    Specifications 6.2.3.1, ``Independent Safety Engineering Group (ISEG) 
    Function;'' 6.2.3.4, ``ISEG Records;'' 6.4.1, ``Training;'' and 
    6.5.2.2, ``Nuclear Review and Audit Group (NRAG) Composition'' are 
    editorial changes reflecting recent administrative/organizational 
    changes which occurred at Clinton Power Station.
        Date of issuance: November 29, 1993
        Effective date: Immediately, to be implemented within 30 days.
        Amendment No.: 86
        Facility Operating License No. NPF-62. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 18, 1993 (58 FR 
    43927) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 29, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library District, 310 N. Quincy Street, Clinton, Illinois 61727
    
    Indiana Michigan Power Company, Docket No. 50-316, Donald C. Cook 
    Nuclear Plant, Unit No. 2, Berrien County, Michigan
    
        Date of application for amendment: April 16, 1993, as supplemented 
    September 28 and December 3, 1993
        Brief description of amendment: The amendment revises Technical 
    Specifications to allow certain tests normally designated as 18-month 
    surveillances to be delayed until the next refueling outage scheduled 
    to begin August 6, 1994.
        Date of issuance: December 22, 1993
        Effective date: December 22, 1993
        Amendment No.: 158
        Facility Operating License No. DPR-74. Amendments revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41505) The supplemental letters provided clarifying information which 
    did not change the staff's initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated December 22, 1993. 
    No significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: June 7, 1993
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3/4.8.1, ``AC Sources-Operating,'' and associated 
    Bases to eliminate unnecessary diesel generator testing when a diesel 
    generator or an offsite power source becomes inoperable. The amendment 
    is intended to increase diesel generator reliability and the overall 
    level of plant safety by reducing the stresses on the diesel generators 
    caused by unnecessary testing. The amendment also makes additional 
    changes to TS 3/4.8.1 to further enhance diesel generator reliability 
    and incorporate certain administrative changes.
        Date of issuance: December 15, 1993
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 54
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36440) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 15, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: November 11, 1992, as supplemented by 
    letters dated July 2, 1993, and November 24, 1993.
        Description of amendment request: The amendment modifies the 
    Seabrook Station Technical Specifications to allow the use of either 
    the fixed incore detector system or the movable incore detector system 
    to perform technical specification surveillances. Specifically, the 
    amendment modifies Technical Specification sections 3.1.3, 4.2.2, 
    4.2.3, 4.2.4, and 3.3.3.
        Date of issuance: December 22, 1993
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 27
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 3, 1993 (58 FR 
    7002). The licensee's letters dated July 2, 1993, and November 24, 
    1993, provide additional information and clarification to the 
    application but do not change the initial proposed no significant 
    hazards consideration determination and do not provide information 
    outside the scope of the original Federal Register notice. The 
    licensee's November 24, 1993, letter provides a commitment to acquire, 
    through the end of Cycle 4, a limited number of flux maps using the 
    movable incore detector system for comparison to flux maps obtained 
    using the fixed incore detector system. Additionally, the licensee 
    committed to provide a report to the NRC at the end of Cycle 4 
    regarding comparison of the data obtained from both systems. The NRC's 
    approval of the requested TS changes is conditioned upon the licensee's 
    implementing the commitment. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated December 22, 1993. 
    No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 47 
    Front Street, Exeter, New Hampshire 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: March 19, 1993
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) to reflect staff positions and improvements to the 
    TS in response to Generic Letter 90-06, ``Resolution of Generic Issue 
    70, `Power-Operated Relief Valve and Block Valve Reliability, and 
    Generic Issue 94, `Additional Low-Temperature Overpressure Protection 
    for Light Water Reactors.''' Generic Issue 94 was closed out by 
    Amendment 80 dated July 12, 1993. With the issuance of this TS 
    amendment, we consider the licensee's response to Generic Letter 90-06 
    and Generic Issue 70 (TAC No. M77362) complete for the Millstone 
    Nuclear Power Station, Unit No. 3.
        Date of issuance: December 16, 1993
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 88
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 9, 1993 (58 FR 
    32388) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 16, 1993. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    Pennsylvania Power and Light Company, Docket No. 50-387, 
    Susquehanna Steam Electric Station, Unit 1, Luzerne County, 
    Pennsylvania
    
        Date of application for amendment: July 21, 1993
        Brief description of amendment: The amendment revised the Technical 
    Specifications to modify the requirement for acquisition of baseline 
    data on single-loop operation from during startup testing following 
    each refueling outage to at least once per 18 months.
        Date of issuance: December 10, 1993
        Effective date: December 10, 1993
        Amendment No.: 131
        Facility Operating License No. NPF-14: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41509) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 10, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Portland General Electric Company, et al., Docket No. 50-344, 
    Trojan Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: April 1, 1993 as supplemented 
    June 9 and August 5, 1993.
        Brief description of amendment: This amendment relocates the 
    Radiological Effluent Technical Specifications (RETS) to the Offsite 
    Dose Calculation Manual (ODCM) and Process Control Program (PCP) in 
    accordance with NRC staff Generic Letter 89-01, and changes the 
    required frequency for submittal of the radioactive Effluent Release 
    Report from semiannual to annual in accordance with 10 CFR 50.36(a).
        Date of issuance: December 6, 1993
        Effective date: 30 days from date of issuance
        Amendment No.: 193
        Facility Operating License No. NPF-1: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36442) The supplements proposed additional changes and clarification to 
    the TS regarding the frequency of effluent reporting. The changes were 
    within the scope of the action described in the notice and did not 
    change the initial no significant hazards consideration determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated December 6, 1993. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: September 25, 1992
        Brief description of amendment: The amendment to the Technical 
    Specifications (TSs) deletes the surveillance requirements for the 
    iodine analyzer portion of the drywell atmosphere Continuous Atmosphere 
    Monitoring system from TS Table 4.6-2 and makes accompanying changes to 
    TS Bases Section 3.6/4.6.D. These changes are consistent with the 
    guidance in Regulatory Guide 1.45, ``Reactor Coolant Boundary Leakage 
    Detection Systems.''
        Date of issuance: December 9, 1993
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 200
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 25, 1993 (58 FR 
    16229) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 9, 1993. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: May 26, 1992
        Brief description of amendments: These amendments increase the 
    shutdown margin requirements for the current operating cycle at both 
    units; reduce the containment pressure high-high setpoint and allowable 
    value; and change the containment spray system, containment fan cooler 
    and service water system response times. These changes were 
    necessitated by the discovery of containment fan cooler unit and 
    containment spray system response times greater than originally assumed 
    for Loss of Coolant Accident (LOCA) or Main Steam Line Break (MSLB) 
    analysis, and auxiliary feedwater system flow greater than assumed for 
    the MSLB analysis.
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993
        Amendment Nos. 149 and 127
        Facility Operating License Nos. DPR-70 and DPR-75. These amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 19, 1992 (57 FR 
    37571) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 16, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: June 28, 1991
        Brief description of amendment: The amendment revised Technical 
    Specification 3.5.1 to add a required action to periodically monitor 
    alternative indication if one or both automatic depressurization system 
    (ADS) safety related instrument air header(s) low pressure alarm system 
    instrumentation channels become inoperable.
        Date of issuance: December 13, 1993
        Effective date: December 13, 1993
        Amendment No.: 52
        Facility Operating License No. NPF-58. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 7, 1991 (56 FR 
    37590) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 13, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: March 19, 1991
        Brief description of amendment: The amendment revised Technical 
    Specification Table 3.3.3-1 to make the required actions for the 
    automatic depressurization system (ADS) consistent with the as-built 
    configuration of the system. An editorial change to Action statement 32 
    was added to this amendment to make Action statement 32 consistent with 
    Action statements 30 and 33.
        Date of issuance: December 17, 1993
        Effective date: December 17, 1993
        Amendment No.: 53
        Facility Operating License No. NPF-58. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 15, 1991 (56 FR 
    22480) Additional clarifying information was provided verbally by the 
    utility on November 5, 1993, that did not change the initial proposed 
    no significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated December 17, 1993. No significant hazards consideration comments 
    received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: November 9, 1992 as supplemented 
    on November 22, 1993
        Brief description of amendment: The amendment revises the Technical 
    Specifications to allow the de-energization of the borated water 
    storage tank outlet isolation valves in the open position during 
    operational Modes 1, 2, 3, and 4.
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993
        Amendment No. 182
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 12, 1993 (58 FR 
    28061) The supplemental letter provided additional information that did 
    not change the proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a safety evaluation dated December 16, 1993. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: August 1, 1991
        Brief description of amendment: The amendment revises the Technical 
    Specification Sections 3.3.3.6, 3.6.4.1, 4.11.2.5, 6.2.2, and Tables 
    3.3-4 and 3.3-10 to correct typographical errors and make editorial 
    changes.
        Date of issuance: December 21, 1993
        Effective date: December 21, 1993
        Amendment No.: 86
        Facility Operating License No. NPF-30. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 18, 1991 (56 
    FR 47244) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated December 21, 1993. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity For a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By February 4, 1994, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Commonwealth Edison Company, Docket No. STN 50-456, Braidwood 
    Station, Unit 1, Will County, Illinois
    
        Date of application for amendment: November 12, 1993, as 
    supplemented by letters dated November 18 and December 6, 1993
        Brief description of amendment: The amendment changes the existing 
    technical specifications (TS) by adding a footnote to TS 4.4.5.0 to 
    address steam generator (SG) operability requirements. The change 
    references an unscheduled inspection of the 1C SG which occurred due to 
    a tube leak in that SG. The amendment was required because the 
    circumstances of the inspection were not covered by the existing TS 3/
    4.4.5. It will allow SG operability requirements to be satisfied until 
    the next SG inservice inspection, scheduled to begin no later than 
    March 5, 1993.
        Date of issuance: December 16, 1993
        Effective date: December 16, 1993
        Amendment No.: 43
        Facility Operating License No. NPF-72. The amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated December 16, 1993.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        Local Public Document Room location: Wilmington Township Public 
    Library, 201 S. Kankakee Street, Wilmington, Illinois 60481.
        NRC Project Director: James E. Dyer
        Dated at Rockville, Maryland, this 28th of December 1993.
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects - III/IV/V, Office of 
    Nuclear Reactor Regulation
    [Doc. 94-53 Filed 1-4-94; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
01/05/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X94-10105
Dates:
December 14, 1993
Pages:
615-639 (25 pages)
Docket Numbers:
Federal Register: January 5, 1994