X95-11011. Biweekly Notice  

  • [Federal Register Volume 60, Number 196 (Wednesday, October 11, 1995)]
    [Notices]
    [Pages 52926-52943]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X95-11011]
    
    
    
    =======================================================================
    -----------------------------------------------------------------------
    
    [[Page 52927]]
    
    
    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating LicensesInvolving 
    No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from September 16, through September 28, 1995. 
    The last biweekly notice was published on Septmeber 27, 1995 (60 FR 
    49929).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By November 10, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one 
    
    [[Page 52928]]
    contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: August 10, 1995
        Description of amendment request: The proposed amendment will add a 
    footnote to Technical Specification (TS) Section 3/4.4.3, 
    ``Pressurizer,'' to allow the pressurizer level to be controlled, 
    outside of the programmed level, between 25 to 50 percent, plus or 
    minus 5 percent in Mode 3 when the reactor coolant system is borated to 
    the required Mode 5 concentrations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ...The proposed change does not involve an SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The design basis accidents analyzed in Mode 3 are steam line 
    break, control rod withdrawal from subcritical, boron dilution and 
    control rod ejection. Of these four analyzed accidents, the relaxing 
    of the pressurizer level requirement can only impact the steam line 
    break accident analyses. The initial pressurizer level can impact 
    the timing of the safety injection signal and the subsequent boron 
    addition from the HPSI [high pressure safety injection] system. The 
    proposed change requires that the boron concentration be equal to 
    the Mode 5 required concentration in order for the pressurizer level 
    to be higher than the current requirement. The Mode 5 boron 
    concentration ensures that there is sufficient negative reactivity 
    in the core due to boron that a steam line break from this condition 
    would not need the boron addition from the HPSI system and would be 
    bounded by the design basis analyses. Thus the proposed change 
    cannot increase the probability or consequences of the design basis 
    accidents.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed change only modifies the Mode 3 pressurizer level 
    requirement. This change does not impact the lower bound but 
    provides flexibility to the plant operators in the maximum 
    pressurizer level. The upper limit still provides margin to 
    pressurizer overfill. This cannot cause an accident nor introduce a 
    new type of malfunction. The modified level would allow for a higher 
    initial pressurizer level in Mode 3. This higher level is already 
    used in the accident analyses which result in an increase in 
    pressurizer level. Therefore, the change does not modify the plant's 
    response to accidents.
        3. Involve a significant reduction in the margin of safety.
        The proposed change is consistent with or bounded by the design 
    basis analyses. The higher shutdown margin required in order to 
    relax the upper bound of the pressurizer level assures that a steam 
    line break from these conditions is bounded by the design basis 
    analyses. Therefore, the proposed change cannot impact the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: September 1, 1995
        Description of amendment request: Generic Letter 88-16 provided 
    guidance on removing cycle-specific parameters which are calculated 
    using NRC-approved methodologies from the Technical Specifications 
    (TS). The parameters are replaced in the TS with a reference to a named 
    report which contains the parameters, and a requirement that the 
    parameters remain within the limits specified in the report. The 
    proposed changes incorporate NRC-approved methodologies, approved 
    revisions to previously approved methodologies, or republished versions 
    of previously approved methodologies into Section 6.9.2 of the Oconee 
    TS. The limits to which these methodologies are applied are 1) Axial 
    Power Imbalance Protective Limits and Variable Low RCS Pressure 
    Protective Limits, 2) Reactor Protective System Trip Setting Limits for 
    the Flux/Flow/Imbalance and Variable Low Reactor Coolant System 
    Pressure Trip functions, and 3) Power Imbalance Limits. Since the 
    proposed changes only incorporate NRC-approved methodologies into the 
    TS, the licensee proposed that the changes are administrative in nature 
    and can be 
    
    [[Page 52929]]
    assumed to have no impact, or potential impact, on the health and 
    safety of the public.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes will not create a significant hazards 
    consideration, as defined by 10 CRF 50.92, because:
        1) The proposed changes will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes are administrative in nature, and do not 
    affect any system, procedure, or manipulation of any equipment which 
    could affect the probability or consequences of any accident.
        2) The proposed changes will not create the possibility of any 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are administrative in nature, and cannot 
    introduce any new failure mode or transient which could create any 
    accident.
        3) The proposed changes will not involve a significant reduction 
    in a margin of safety.
        The proposed changes are administrative in nature, and will not 
    affect any operating parameters or limits which could result in a 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: November 9, 1994, as supplemented by 
    letter dated August 4, 1995
        Description of amendment request: This supplement revises the 
    licensee's November 9, 1994, application by updating the request to 
    reflect implementation of the Improved Standard Technical 
    Specifications on March 20, 1995, and by deleting the request for a 
    definition of the term RECENTLY IRRADIATED FUEL. The proposed amendment 
    revises those specifications associated with various engineered safety 
    feature systems following a design basis fuel handling accident. The 
    proposed changes affect conditions where irradiated fuel is handled in 
    the primary or secondary containment and when fuel is handled over the 
    reactor vessel with fuel in the vessel. These changes are based on a 
    recent re-analysis of the fuel handling accident for Grand Gulf Nuclear 
    Station (GGNS).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not significantly increase the 
    probability or consequences of an accident previously evaluated.
        A new term to describe irradiated fuel is used to establish 
    operational conditions where specific activities represent 
    situations where significant radioactive releases can be postulated. 
    These operational conditions are consistent with the design basis 
    analysis. Because the equipment affected by the revised operational 
    conditions is not considered an initiator to any previously analyzed 
    accident, inoperability of the equipment cannot increase the 
    probability of any previously evaluated accident. The proposed 
    requirements in conjunction with existing administrative controls on 
    light loads, bounds the conditions of the current design basis fuel 
    handling accident analysis which concludes that the radiological 
    consequences are within the acceptance criteria of NUREG 0800, 
    Section 15.7.4 and General Design Criteria 19. Therefore, the 
    proposed changes do not significantly increase the probability or 
    consequences of any previously evaluated accident.
        Based on the above, the proposed changes do not significantly 
    increase the probability or consequences of any accident previously 
    evaluated.
        2. The proposed changes would not create the possibility of a 
    new or different kind of accident from any previous analyzed.
        The new term to describe irradiated fuel is used to establish 
    operational conditions where specific activities represent 
    situations where significant radioactive releases can be postulated. 
    These operational conditions are consistent with the design basis 
    analysis. The proposed changes do not introduce any new modes of 
    plant operation and do not involve physical modification of the 
    plant. Therefore, the proposed changes do not create the possibility 
    of a new or different kind of accident from any previous analyzed.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The new term to describe irradiated fuel is used to establish 
    operational conditions where specific activities represent 
    situations where significant radioactive releases can be postulated. 
    These operational conditions are consistent with the design basis 
    analysis and are established such that the radiological consequences 
    are at or below the current GGNS licensing limit. Safety margins and 
    analytical conservatisms have been evaluated and are well 
    understood. Substantial margins are retained to ensure that the 
    analysis adequately bounds all postulated event scenarios. The 
    proposed change only eliminates the excess margin from the analysis. 
    The current margin of safety is retained.
        Specifically, the margin of safety for the fuel handling 
    accident is the difference between the 10 CFR 100 limits and the 
    licensing limit defined by NUREG 0800, Section 15.7.4. With respect 
    to the control room personnel doses, the margin of safety is the 
    difference between the 10 CFR 100 limits and the licensing limit 
    defined by 10 CFR 50, Appendix A, Criterion 19 (GDC 19). Excess 
    margin is the difference between the postulated doses and the 
    corresponding licensing limit.
        The proposed applicability continues to ensure that the
        whole-body and thyroid dose at the exclusion area and low 
    population zone boundaries as well as control room, doses are at or 
    below the corresponding licensing limit. The margin of safety is 
    unchanged; therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        Therefore, the proposed changes do not result in a significant 
    reduction in a margin of safety.
        Based on the above evaluation, operation in accordance with the 
    proposed amendment involves no significant hazards considerations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of amendment request: July 19, 1995
        Description of amendment request: The proposed amendment reduces 
    requirements associated with the exercise frequency of control element 
    assemblies from once per 31 days to once per 92 days.
        Basis for proposed no significant hazards consideration 
    determination: 
    
    [[Page 52930]]
    As required by 10 CFR 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        1. Does not Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        Changing the frequency of the control element assemblies (CEA) 
    exercise test surveillance introduces no new failure mechanism for 
    the system, so the consequences of a postulated stuck CEA are no 
    different than those previously evaluated.
        As explained in NUREG-1366, ``Improvements to Technical 
    Specifications Surveillance Requirements,'' the purpose of this test 
    is to identify immovable CEAs. NUREG-1366 goes on to explain that 
    the majority of CEA problems are identified during the performance 
    of startup physics testing and during CEA withdrawal for startup, 
    not during the exercise test. The incidence of electrical 
    malfunctions which will still allow CEA insertion is much greater 
    than the incidence of mechanically bound CEAs. As stated in NUREG-
    1366, there has only been one incidence of multiple CEAs failing to 
    fully insert upon a reactor trip (Point Beach Nuclear Plant, May 
    1985) and in this case the two affected CEAs partially inserted. 
    Based on this history, simply reducing the test frequency will not 
    increase the probability of a stuck CEA.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. Does Not Create the Possibility of a New or Different Kind of 
    Accident from any Previously Evaluated.
        Because the proposed change does not alter the design, 
    configuration, or method of operation of the plant, it does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. Does Not Involve a Significant Reduction in the Margin of 
    Safety.
        The proposed change does not alter the acceptance criteria of 
    any surveillance requirements, alter any assumptions used in 
    accident analysis, change any actuation setpoints, nor allow 
    operations in any configuration not previously evaluated. This 
    change in surveillance frequency is based on a satisfactory 
    operating history of CEAs. Additionally, the number of problems 
    created by this test when compared with the number of problems 
    identified by this test indicate that reducing the test frequency 
    will have no adverse impact on the continued safe operation of the 
    unit.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        Therefore, based upon the reasoning presented above and the 
    previous discussion of the amendment request, Entergy Operations had 
    determined that the requested change does not involve a significant 
    hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: September 11, 1995
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications (TS) to incorporate 
    line-item improvements to Specifications 3/4.8.1, ``Electrical Power 
    Systems-A.C. Sources,'' and the associated BASES. The licensee stated 
    that the proposed changes are consistent with the guidance provided by 
    the NRC in GL 93-05, ``Line-Item Technical Specifications Improvements 
    to Reduce Surveillance Requirements for Testing During Power 
    Operation,'' and the corresponding recommendations contained in NUREG-
    1366, ``Improvements to Technical Specifications Surveillance 
    Requirements.''
        In addition, line-item improvements are proposed following the 
    guidance in GL 94-01, ``Removal of Accelerated Testing and Special 
    Reporting Requirements for Emergency Diesel Generators.'' The 
    implementation of a maintenance program for monitoring and maintaining 
    Emergency Diesel Generator (EDG) performance for Turkey Point Units 3 
    and 4, consistent with the provisions of 10 CFR 50.65 ``Requirements 
    for Monitoring the Effectiveness of Maintenance at Nuclear Power 
    Plants'' and the associated guidance of Regulatory Guide (RG) 1.160 
    will be met by FPL within 90 days following issuance of the proposed 
    amendments.
        The licensee also requested to revise the current wording used in 
    the Turkey Point Units 3 and 4 TS to require testing of remaining 
    required diesel generators ``[i]f the diesel generator became 
    inoperable due to any cause other than planned preventative 
    maintenance...''. The licensee requested that TS 3.8.1.1, ACTION 
    statements b. and c. be amended such that the word 'preventative' is 
    deleted. Deleting this wording will reduce unnecessary testing of 
    diesel generators as a result of planned corrective maintenance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The license amendments proposed for Turkey Point Units 3 and 4 
    will incorporate line-item Technical Specification (TS) improvements 
    for Emergency Diesel Generators (EDG) pursuant to guidance provided 
    in Generic Letters (GL) 93-05 and 94-01. The EDGs are not accident 
    initiators, the proposed TS changes do not involve any assumptions 
    relative to accident initiators in the plant safety analyses, and 
    therefore the proposed amendments will not impact the probability of 
    occurrence for accidents previously analyzed.
        The EDG line-item TS improvements associated with GL 93-05 are 
    based on recommendations designed to remove unwarranted requirements 
    for testing during power operation and other factors that are 
    counter-productive to safety in terms of equipment degradation and 
    availability. These recommendations resulted from a comprehensive 
    study of industry-wide EDG surveillance requirements and subsequent 
    findings reported by the NRC in NUREG-1366. The proposed amendments 
    are consistent with the guidance of GL 93-05 for implementing such 
    recommendations as well as contemporary licensing actions by the NRC 
    on other light water reactors.
        Similarly, GL 94-01 provides guidance for a line-item TS 
    improvement that will remove accelerated testing requirements from 
    the TS provided that the licensee commits to a maintenance program 
    for monitoring and maintaining EDG performance that includes the 
    applicable provisions of the maintenance rule (10 CFR 50.65). Such a 
    program will further assure EDG availability. Since the availability 
    of EDGs is assumed in certain success paths for mitigating analyzed 
    accidents, an improvement in EDG availability will enhance accident 
    mitigation capabilities.
        Therefore, operation of the facility in accordance with the 
    proposed amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendments incorporate line-item TS and other 
    improvements to EDG surveillance testing requirements, and will not 
    change the physical plant or the modes of plant operation defined in 
    the Facility License. The changes do not involve the addition or 
    modification of equipment, nor do they alter the design or methods 
    of operation of plant systems. Plant configurations that are 
    prohibited by TS will 
    
    [[Page 52931]]
    not be created by the amendments. Therefore, operation of the facility 
    in accordance with the proposed amendment would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The proposed amendments are designed to improve EDG availability 
    by eliminating unwarranted surveillance testing. The currently 
    specified surveillance intervals are not changed, except to delete 
    the requirement for accelerated testing under certain circumstances. 
    The proposed changes do not otherwise alter the basis for any 
    Technical Specification that is related to the establishment of, or 
    the maintenance of a nuclear safety margin. Therefore, operation of 
    the facility in accordance with the proposed amendment would not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of amendment request: July 24, 1995
        Description of amendment request: The proposed amendment would 
    modify Technical Specification 3.6.C to allow up to 7 days to restore 
    low pressure safety injection (LPSI) pump subsystem operability, and up 
    to 24 hours to restore safety injection tank (SIT) operability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The staff's review is 
    presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The LPSI system is designed primarily to 
    mitigate the consequences of a large loss-of-coolant accident 
    (LOCA). Inoperable LPSI components are not accident initiators in 
    any accident previously evaluated, and the proposed change does not 
    affect any of the assumptions relative to accident initiators in the 
    plant's safety analysis. Probabilistic safety analysis (PSA) methods 
    were used to fully evaluate the extension of the LPSI system allowed 
    outage time (AOT). The licensee asserts that the results of these 
    analyses show no significant increase in the consequences of an 
    accident previously evaluated. The SITs were designed to mitigate 
    the consequences of a LOCA. The proposed amendment does not affect 
    any of the assumptions used in the deterministic LOCA analysis. 
    Probabilistic safety analysis methods were used to fully evaluate 
    the effect of the SIT allowable outage time (AOT). The licensee 
    asserts that the results of these analyses show no significant 
    increase in the consequences of an accident previously evaluated. 
    Thus, there is no significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The proposed amendment does not change the design, 
    physical configuration, or modes of operation of the plant. Plant 
    configurations that are prohibited by TS will not be created by this 
    proposed amendment. Thus, the proposed amendment does not create the 
    possibility or consequences of an accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety. The proposed amendment does not 
    affect the limiting conditions for operation or the bases used in 
    the deterministic analyses to establish the margin of safety. The 
    licensee asserts that PSA methods were used to evaluate these 
    changes and demonstrate that the changes are either risk neutral or 
    risk beneficial. Thus, the proposed amendment does not involve a 
    significant reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that this amendment request involves no significant hazards 
    determination.
        Local Public Document Room location:  Wiscasset Public Library, 
    High Street, P.O. Box 367, Wiscasset, ME 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011
        NRC Project Director: Phillip F. McKee
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of amendment request: August 8, 1995
        Description of amendment request: The proposed amendment would 
    modify the definition of Transthermal (Condition 4), Hot Shutdown 
    (Condition 5), and Hot Standby (Condition 6) reactor operating 
    conditions. The Transthermal and Hot Shutdown conditions are modified 
    to establish an applicable range of subcriticality and be consistent 
    with other Definitions. The wording of Hot Standby is modified to 
    remove reference to control rod position, consistent with NUREG-1432, 
    Standard Technical Specifications for Combustion Engineering Plants, 
    Revision 1 dated April 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The staff's review is 
    presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The changes to these Definitions are 
    administrative in nature. The Transthermal and Hot Shutdown 
    conditions are changed by adding ``at least'' to establish a range 
    of subcriticality. The current Definitions for the Transthermal and 
    Hot Shutdown conditions set one minimum value for subcriticality; 
    the change to these two Definitions would allow a range of values 
    for subcriticality. All values of subcriticality that may be 
    established by this change are below the current Definitions (more 
    subcritical). The change to the wording of Hot Standby removes 
    confusion about the Conditions during which control rods may be 
    withdrawn and is consistent with current NRC guidance. All current 
    plant analyses, requirements and acceptance criteria on 
    subcriticality conditions remain in effect. The changes to these 
    Definitions have no impact on event probabililty. Thus, the proposed 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The proposed amendment clarifies the subject Definitions. 
    Limits on subcriticality requirements are unaffected, as are 
    reactivity transients previously evaluated. Plant procedures 
    currently require that minimum values for subcriticality be 
    established. All values of subcriticality that may be established by 
    this change are below the current Definitions (more subcritical). 
    Further, the change to the wording of Hot Standbyis consistent with 
    current NRC guidance. Thus, the proposed amendment does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety. Adding the words ``at least'' to 
    the Transthermal and Hot Shutdown conditions establishes a range of 
    subcriticality to the 
    
    [[Page 52932]]
    Definitions for these terms. All values of subcriticality are below 
    (more subcritical) than the current value, thus the margin of safety 
    is increased. All current plant analyses, requirements and 
    acceptance criteria on subcriticality conditions remain in effect. 
    The change to the wording of Hot Standby removes confusion about the 
    Conditions during which control rods may be withdrawn and is 
    consistent with current NRC guidance. Thus, there is no significant 
    reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that this amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011
        NRC Project Director: Phillip F. McKee
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of amendment request: August 30, 1995
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) 1.3.A, Reactor Core, to allow the 
    use of fuel rods clad with zirconium alloy, rather than restrict fuel 
    rod cladding to Zircaloy-4. In addition, the fuel enrichment limit 
    described in this specification would be changed to more closely agree 
    with the wording found in NUREG-1432, ``Standard Technical 
    Specifications for Combustion Engineering Plants,'' dated April 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The staff's review is 
    presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an acident previously 
    evaluated. Maine Yankee (MY) reload cores containing fuel rods clad 
    with zirconium alloy and having higher fuel enrichments will be 
    analyzed using NRC-approved methods and applicable acceptance 
    criteria. In addition, the impact of fuel assembly design changes on 
    fuel storage will be analyzed using NRC-approved methods and 
    acceptance criteria. Compliance with the acceptance criteria for the 
    applicable analysis for a given core design must be determined for 
    each core prior to reloading. The material used to clad the fuel and 
    the fuel enrichment are only two of the factors considered in this 
    determinination. The application of approved methods ensures that 
    all appropriate variables are addressed and their acceptance 
    criteria satisfied. Thus, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The determination of compliance with the acceptance 
    criteria of the approved safety evaluation for any given core reload 
    design is performed for each MY reload core prior to loading. In 
    addition, determination of compliance with the acceptance criteria 
    of the approved safety evaluation for fuel storage is performed for 
    each core prior to receipt of the fuel. The use of approved methods 
    and their acceptance criteria ensures that new or different 
    accidents will not be encountered by the use of fuel rods clad with 
    zirconium alloy and having higher fuel enrichments. Further, the 
    proposed change does not involve any altertions to plant equipment 
    that would affect any operational modes or accident precursors. 
    Finally, the proposed change does not involve, or require secondary 
    involvement of, any equipment important to safety. Thus the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety. Maine Yankee reload cores containing fuel 
    rods clad with zirconium alloy and having higher fuel enrichments 
    will be analyzed using NRC-approved methods and applicable 
    acceptance criteria. Safety evaluations performed for each core 
    reload ensure that the core design meets appropriate safety 
    assessment acceptance criteria. In addition, the impact of fuel 
    assembly design changes on fuel storage also will be analyzed using 
    NRC-approved methods and aceptance criteria. Application of the 
    approved methods ensures that the requirements of MY TS 1.1, Fuel 
    Storage, are achieved. Because these requirements are not changed, 
    the margin of safety remains the same. Thus there is no significant 
    reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that this amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011
        NRC Project Director: Phillip F. McKee
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine 
    YankeeAtomic Power Station, Lincoln County, Maine
    
        Date of amendment request: August 31, 1995
        Description of amendment request: The proposed amendment would 
    relocate fire protection requirements from the Maine Yankee (MY) Atomic 
    Power Station Technical Specifications (TS) to other, licensee-
    controlled documents. The proposed amendment is consistent with the 
    guidance of U.S. NRC Generic Letters 86-10, Implementation of Fire 
    Protection Requirements, and 88-12, Removal of Fire Protection 
    Requirements from the Technical Specifications.
        Basis for proposed no significant hazards consideration 
    etermination: As required by 10 CFR 50.91(a), the licensee has provided 
    its analysis if the issue of no significant hazards consideration. The 
    NRC staff has reviewed the licensee's analysis against the standards of 
    10 CFR 50.92(c). The NRC staff's review is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The proposed change is administrative and consistent with 
    the guidance provided by the U.S. NRC. Removing fire protection 
    requirements from the TS does not affect any fire protection 
    equipment, or involve any physical modifications to plant 
    structures, systems or components. The proposed change is not 
    associated with accident initiation or mitigation and cannot affect 
    the probability of occurrence of an accident, or increase the 
    consequences of an accident. The licensee's fire protection plan 
    contains the relocated requirements.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The proposed change introduces no new mode of plant 
    operation, does not involve physical modification of any structure, 
    system or component, and does not affect the function, operation or 
    surveillance requirements of any equipment necessary for safe 
    operation or shutdown. Further, the proposed change does not involve 
    any change to equipment setpoints or operating parameters. The 
    proposed change is administrative in nature. Existing plant fire 
    protection equipment requirements are retained. Thus, the proposed 
    change does not create the possibility for a new or different kind 
    of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety. No margins of safety established by system or 
    component design, or verified by testing to ensure operability of 
    fire protection systems or components, are affected. Fire protection 
    requirements currently found in the TS will be relocated in their 
    entirety to the Maine Yankee Fire Protection Plan. Any future 
    
    [[Page 52933]]
    changes to the Plan will be evaluated in accordance with the 
    requirements of 10 CFR 50.59, Changes, tests and experiments. Thus 
    the proposed change does not involve a significant reduction in a 
    margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit Nos. 2, New London, 
    Connecticut
    
        Date of amendment request: September 11, 1995
        Description of amendment request: The proposed changes affect 
    Technical Specification Sections 3.4.8 and 3.9.9, Tables 2.2-1, 3.3-3, 
    3.3-5 and 3.3-8, and Bases Sections 3/4.2.1, 3/4.4.8 and 3/4.11.2.1. 
    These changes combine several different administrative changes which 
    will correct typographical errors, provide clarifications, or make 
    editorial changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
        Pursuant to 10CFR50.92, NNECO has reviewed the proposed changes. 
    NNECO concludes that these changes do not involve a significant 
    hazards consideration since the proposed change satisfies the 
    criteria in 10CFR50.92(c). That is, the proposed changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed changes are administrative in nature and do not 
    result in changes to plant configuration, operation, accident 
    mitigation, or analysis assumptions. Thus, it cannot increase the 
    probability or consequence of an accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes are administrative in nature and do not 
    result in changes to plant configuration, operation, accident 
    mitigation, or analysis assumptions. The intent and application of 
    the proposed specification will not change. Therefore, the proposal 
    does not create the possibility of a new or different kind of 
    accident from any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        Since the proposed change[s] are administrative in nature and do 
    not result in changes to plant configuration, operation, accident 
    mitigation, or analysis assumptions, there is no reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: July 17, 1995
        Description of amendment requests: The proposed amendments would 
    revise the Prairie Island Radiological Effluent Technical 
    Specifications and other sections relating to radiological controls to 
    conform to NUREG-1431, Standard Technical Specifications, Westinghouse 
    Plants, Revision 1, and Generic Letter 89-01, ``Implementation of 
    Programmatic Controls for Radiological Effluent Technical 
    Specifications in the Administrative Controls Section of the Technical 
    Specifications and the Relocation of Procedural Details of RETS to the 
    Offsite Dose Calculation Manual or to the Process Control Program.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The proposed changes are administrative in nature and alter only the 
    format and location of programmatic controls and procedural details 
    relative to radioactive effluents, radiological environmental 
    monitoring, radioactive source leakage testing, solid radioactive 
    wastes, and associated reporting requirements. Existing Technical 
    Specifications containing procedural details on radioactive 
    effluents, radiological environmental monitoring, radioactive source 
    leakage testing, explosive gas monitoring, storage tank radioactive 
    content limits, solid radioactive wastes and associated reporting 
    requirements are being relocated to the Offsite Dose Calculation 
    Manual, Process Control Program or other new programs as 
    appropriate. Compliance with applicable regulatory requirements will 
    continue to be maintained. In addition, the proposed changes do not 
    alter the conditions or the assumptions in any of the previous 
    accident analyses. Since the previous accident analyses remain 
    bonding, the radiological consequences previously evaluated are not 
    adversely affected by the proposed changes.
        Therefore, the probability or consequences of an accident 
    previously evaluated are not affected by any of the proposed 
    amendments.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The proposed changes do not involve any change to the configuration 
    or method of operation of any plant equipment. Accordingly, no new 
    failure modes have been defined for any plant system or component 
    important to safety nor has any new limiting single failure been 
    identified as a result of the proposed changes. Also, there will be 
    no change in types or increase in the amounts of any effluents 
    released offsite.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be 
    created.
        3. The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The proposed changes do not involve a significant reduction in a 
    margin of safety. The proposed changes do not involve any actual 
    change in the methodology used in the control of radioactive 
    effluents, radioactive sources, solid radioactive wastes, or 
    radiological environmental monitoring. These changes are considered 
    administrative in nature and provide for the relocation of 
    procedural details outside of the technical specifications but add 
    appropriate administrative controls to provide continued assurance 
    of compliance to applicable regulatory requirements. These proposed 
    changes also comply with the guidance contained in Generic Letter 
    89-01 and the Standard Technical Specifications.
        Therefore, it can be concluded a significant reduction in the 
    margin of safety would not be involved.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
    
    [[Page 52934]]
    
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick 
    Generating Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of amendment request: June 19, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Section 2.1, ``Safety Limits,'' to 
    change the Minimum Critical Power Ratio Safety Limit due to the use of 
    General Electric 13 fuel product line.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The derivation of the revised GE13 [General Electric] Minimum 
    Critical Power Ratio (MCPR) Safety Limit for incorporation into the 
    Technical Specifications, and its use to determine cycle-specific 
    thermal limits have been performed using NRC-approved methods within 
    the existing design and licensing basis, and cannot increase the 
    probability or severity of an accident.
        The basis of the MCPR Safety Limit calculation is to ensure that 
    greater than 99.9% of all fuel rods in the core avoid boiling 
    transition if the limit is not violated. The new MCPR Safety Limit 
    preserves the existing margin to transition boiling and fuel damage 
    in the event of a postulated accident.
        All design bases of the MCPR Safety Limit calculation apply to 
    GE13 fuel in the same manner that they have applied to previous fuel 
    designs. The probability of fuel damage is not increased.
        Therefore, the proposed TS change does not involve an increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The MCPR Safety Limit for the GE13 fuel design is a Technical 
    Specification numerical value, designed to ensure that fuel damage 
    from transition boiling does not occur as a result of the limiting 
    postulated accident. It cannot create the possibility of any new 
    type of accident. The new Minimum Critical Power Ratio (MCPR) Safety 
    Limit is calculated using NRC-approved methods and has the same 
    calculational basis as the MCPR Safety Limit for other GE fuel 
    designs currently used at LGS [Limerick Generating Station] Unit 1.
        Therefore, the proposed TS change does not create the 
    possibility of a new or different kind of accident, from any 
    accident previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        The following TS Bases were reviewed for potential reduction in 
    the margin of safety:
        2.1 ``Safety Limits''
        3/4.2.1 ``Average Planar Linear Heat Generation Rate''
        3/4.2.3 ``Minimum Critical Power Ratio''
        3/4.2.4 ``Linear Heat Generation Rate''
        3/4.4.1 ``Recirculation System''
        3/4.9 ``Refueling Operations''
        The margin of safety as defined in the TS Bases will remain the 
    same. The new Minimum Critical Power Ratio (MCPR) Safety Limit is 
    calculated using NRC approved methods which are in accordance with 
    the current fuel design and licensing criteria. The MCPR Safety 
    Limit for GE13 fuel remains high enough to ensure that greater than 
    99.9% of all fuel rods in the core will avoid boiling transition if 
    the limit is not violated, thereby preserving the fuel cladding 
    integrity.
        Therefore, the proposed TS change does not involve a reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: John F. Stolz
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: September 14, 1995
        Description of amendment request: The amendments change the 
    Technical Specifications (TS) by removing the Reactor Enclosure and 
    Refueling Area Secondary Containment Isolation Valve Tables 3.6.5.2.1-1 
    and 3.6.5.2.2-1 from TS in accordance with NRC Generic Letter (GL) 91-
    08, ``Removal of Component Lists from Technical Specifications.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes will remove component tables from TS. The 
    component lists will be retained in licensee controlled documents 
    (UFSAR [Updated Final Safety Analysis Report] and a plant procedure) 
    which will be maintained under the requirements of TS Administrative 
    Controls Section 6.0 and the provisions of 10 CFR 50.59. Since any 
    changes to licensee controlled documents are required to be 
    evaluated per 10 CFR 50.59, no increase (significant or 
    insignificant) in the probability or consequences of an accident 
    previously evaluated will be allowed.
        In addition, these proposed changes will not affect any 
    equipment important to safety, in structure or operation. These 
    changes will not alter operation of process variables, structures, 
    systems, or components as described in the safety analysis and 
    licensing basis. The changes will not increase the probability or 
    consequences of occurrence of a malfunction of equipment important 
    to safety previously evaluated in the SAR [Safety Analysis Report].
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes will not alter the plant configuration or 
    change the methods governing normal plant operation. The changes 
    will not impose different operating requirements and adequate 
    control of information will be retained. The changes will not alter 
    assumptions made in the safety analysis and licensing basis. Since 
    the proposed changes cannot cause an accident, and the plant 
    response to the design basis events is unchanged, the changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The proposed changes to remove the component tables from TS have 
    been performed under the guidance of NRC GL 91-08. The component 
    lists will be retained in licensee controlled documents (UFSAR and a 
    plant procedure) which will be maintained under the requirements of 
    TS Administrative Controls Section 6.0 and the provisions of 10 CFR 
    50.59. These changes will not reduce the margin of safety since they 
    have no impact on any safety analysis assumptions. Since any future 
    changes to the removed tables will be evaluated under the 
    requirements of 10 CFR 50.59, no reduction (significant or 
    insignificant) in a margin of safety will be allowed. Therefore, the 
    proposed TS changes do not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    
    
    [[Page 52935]]
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: John F. Stolz
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: May 26, 1995
        Brief description of amendment: The proposed amendment would 
    represent a full conversion from the current Technical Specifications 
    (TSs) to a set of TS based on NUREG-1431, ``Standard Technical 
    Specifications, Westinghouse Plants,'' Revision 0, dated September 
    1993, together with approved travellers used in the issuance of 
    Revision 1, dated April 1995. NUREG-1431 was developed through working 
    groups composed of NRC staff members and industry representatives and 
    has been endorsed by the staff as part of an industry-wide initiative 
    to standardize and improve the TSs. As part of this submittal, the 
    licensee has applied the criteria contained in the Commission's Final 
    Policy Statement on Technical Specification Improvements for Nuclear 
    Power Reactors of July 22, 1993, to the current Ginna TSs, and using 
    NUREG-1431 as a basis, developed a proposed set of improved TSs for 
    Ginna.Date of publication of individual notice in Federal Register: 
    September 26, 1995 (60 FR 49636)
        Expiration date of individual notice: October 26, 1995
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610
    
    Tennessee Valley Authority, Docket No. 50-296, Browns Ferry Nuclear 
    Plant, Unit 3, Limestone County, Alabama
    
        Date of amendment request: September 13, 1995 (TS 368)
        Description of amendment request: The proposed amendment deletes 
    requirements for daily checks for certain instruments that do not have 
    indications, and provides editorial changes.
        Basis for proposed no significant hazards consideration 
    determination:As required by 10 CFR 50.91(a), the licensee has provided 
    its analysis of the issue of no significant hazards consideration, 
    which is presented below:
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed changes are administrative in nature and correct 
    errors that were introduced by previous changes to the TSs. These 
    changes do not affect any of the design basis accidents nor do they 
    involve an increase in the probability or consequences of an 
    accident previously evaluated.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are administrative in nature. These changes 
    do not change the operation or function of the affected 
    instrumentation. The deletion of the RCIC and HPCI instrument checks 
    reflects the actual installed configuration of this instrumentation 
    (no indication) and the change to Table 4.2.C corrects the 
    referenced note for the SRM Upscale function. Therefore, the 
    possibility for an accident or malfunction of a different type than 
    any evaluated previously is not created by this change.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed changes are administrative in nature. The proposed 
    changes to TS Tables 4.2.B and 4.2.C do not affect any acceptable 
    limit of operation, instrument setpoint, or analysis assumption in 
    the TS or Bases. Therefore, this change does not reduce the margin 
    of safety as defined in the basis for any TS.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: August 15, 1995
        Brief description of amendments: The proposed amendment would 
    relocate the Shutdown Margin limits from the Technical Specifications 
    (TSs) to the Core Operating Limits Report. The proposed changes are 
    consistent with the intent of Generic Letter (GL) 88-16 which provides 
    guidelines for the removal of cycle-specific parameter limits from the 
    TSs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes remove cycle-specific parameter limits from 
    the Technical Specifications, add them to the list of limits 
    contained in the Core Operating Limits Report (COLR), and revise the 
    Administrative Controls section of the Technical Specifications. The 
    changes do not, by themselves, alter any of the parameter limits. 
    The changes are administrative in nature and have no adverse effect 
    on the probability of an accident or on the consequences of an 
    accident previously evaluated. The removal of parameter limits from 
    the Technical Specifications does not eliminate the requirement to 
    comply with the parameter limits.
        The parameter limits in the COLR may be revised without prior 
    NRC approval. However, Specification 6.9.1.6c continues to ensure 
    that the parameter limits are developed using NRC-approved 
    methodologies and that applicable limits of the safety analyses are 
    met. While future changes to the COLR parameter limits could result 
    in event consequences which are either slightly less or slightly 
    more severe than the consequences for the same event using the 
    present parameter limits, the differences would not be significant 
    and would be bounded by the requirement of specification 6.9.1.6c to 
    meet the applicable limits in the safety analysis.
        Based on the above, removal of the parameter limits from the 
    Technical Specifications and the addition of these limits the list 
    of limits in the COLR, thus allowing revision of the parameter 
    limits without prior NRC approval, has no significant effect on the 
    probability or consequences of an accident previously evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed changes remove certain parameter limits from the 
    Technical Specifications and add these limits to the list of limits 
    in the COLR, removing the requirement for prior NRC approval of 
    revisions to those parameters. The changes do not add new hardware 
    or change plant operations and therefore cannot initiate an event 
    nor cause an analyzed event to progress differently. Thus, the 
    possibility of a new or different kind of accident is not created.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        The margin of safety, as it relates to a parameter limit, is the 
    difference between the 
    
    [[Page 52936]]
    acceptance criterion for that parameter and its failure value. The 
    proposed changes do not affect the failure values for any system. 
    Through the accident analyses, all relevant event acceptance 
    criteria (as described in the NRC-approved analysis methodologies) 
    are shown to be satisfied; therefore, there is no impact on an event 
    acceptance criteria. Because neither the failure values nor the 
    acceptance criteria are affected, the proposed change has no effect 
    on the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: September 19, 1995
        Description of amendment request: The proposed amendment would make 
    administrative changes to the Kewaunee Nuclear Power Plant (KNPP) 
    Technical Specifications (TS) to improve their clarity and consistency. 
    The proposed amendment includes changes to reflect revisions to 10 CFR 
    Part 20, and changes to correct minor typographical and format 
    inconsistencies as part of an ongoing effort to convert the TS to the 
    WordPerfect format.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The likelihood that an accident will occur is neither increased 
    or decreased by these TS changes. These TS changes will not impact 
    the function or method of operation of plant equipment. Thus, there 
    is not a significant increase in the probability of a previously 
    analyzed accident due to these changes. No systems, equipment, or 
    components are affected by the proposed changes. Thus, the 
    consequences of the malfunction of equipment important to safety 
    previously evaluated in the Updated Safety Analysis Report (USAR) 
    are not increased by these changes.
        The proposed changes are administrative in nature and, 
    therefore, have no impact on accident initiators or plant equipment, 
    and thus, do not affect the probabilities or consequences of an 
    accident.
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        Operation of the facility in accordance with the proposed TS 
    changes would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed changes do not involve changes to the physical 
    plant or operations. Since these administrative changes do not 
    contribute to accident initiation, they do not produce a new 
    accident scenario or produce a new type of equipment malfunction. 
    Also, these changes do not alter any existing accident scenarios; 
    they do not affect equipment or its operation, and thus, do not 
    create the possibility of a new or different kind of accident.
        3. involve a significant reduction in the margin of safety.
        Operation of the facility in accordance with the proposed TS 
    would not involve a significant reduction in a margin of safety. The 
    proposed changes do not affect plant equipment or operation. Safety 
    limits and limiting safety system settings are not affected by these 
    proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: Gail H. Marcus
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: September 14, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 3/4.5.5 to increase the outage time 
    allowed for adjusting the boron concentration of the refueling water 
    storage tank (RWST) from 1 hour to 8 hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The increase in the RWST allowed outage time does not alter the 
    plant configuration or operation. The potential for the RWST boron 
    concentration to be outside the technical specification limits is 
    small because the RWST and its contents are not involved with normal 
    plant operation and are not subject to process variations associated 
    with plant operation.
        The potential causes of boron concentration deviation have been 
    evaluated with the conclusion that any deviation in RWST boron 
    concentration would not be expected to increase significantly during 
    the proposed 7 hour allowed outage time increase.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Increasing the RWST allowed outage time from 1 hour to 8 hours 
    for reasons directly related to boron concentration does not require 
    physical alteration to any plant system and does not change the 
    method by which any safety related system performs its functions. 
    Therefore, the proposed change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Increasing the RWST allowed outage time for reasons directly 
    related to boron concentration does not affect any accident analysis 
    assumptions, initial conditions, or results. The margins of safety 
    reflected in the Wolf Creek Generating Station Technical 
    Specifications are not compromised by the 7 hour allowed outage time 
    increase. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    [[Page 52937]]
    
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois, Docket 
    Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 
    2, Will County, Illinois
    
        Date of amendment request: September 1, 1995
        Description of amendment request: The proposed amendments would 
    revise the present voltage-based repair criteria in the Byron 1 and 
    Braidwood 1 Technical Specifications (TSs). These proposed revisions 
    would raise the lower voltage limit from its present value of 1.0 volt 
    to 3.0 volts; there would no longer be an upper voltage limit.
        The Braidwood 1 TSs were revised by License Amendment No. 54, 
    issued on August 18, 1994, to add voltage-based repair criteria to the 
    existing steam generator (SG) tube repair criteria. The Byron 1 TSs 
    were revised in a similar manner by License Amendment No. 66, issued on 
    October 24, 1994.
        The voltage-based repair criteria in the subject TSs are applicable 
    only to a specific type of SG tube degradation which is predominantly 
    axially-oriented outer diameter stress corrosion cracking (ODSCC). This 
    particular form of SG tube degradation occurs entirely within the 
    intersections of the SG tubes with the tube support plates (TSPs).
        The present voltage values for the ODSCC repair criteria are based 
    on the assumption of a ``free span'' exposure of the SG tube flaw; 
    i.e., no credit is given for any constraint against burst or leakage, 
    which may be provided by the presence of the TSPs. This approach is, in 
    turn, based on the assumption that under postulated accident 
    conditions, the TSPs may be displaced sufficiently by blowdown 
    hydrodynamic loads such that a SG tube flaw which was fully confined 
    within the thickness of the TSP prior to the accident would then be 
    fully exposed. This approach was first advanced by the NRC staff in a 
    draft generic letter issued on August 12, 1994, which was subsequently 
    modified slightly and issued as Generic letter (GL) 95-05, ``Voltage-
    Based Repair Criteria For Westinghouse Steam Generator Tubes Affected 
    by Outside Diameter Stress Corrosion Cracking,'' dated August 3, 1995. 
    The previous license amendments related to the issue of ODSCC were 
    based to a large extent on the draft generic letter cited above.
        The fundamental difference between the pending proposal to raise 
    the lower voltage repair limit to 3.0 volts and the methodology 
    contained in GL 95-05, is that the licensee proposes to install certain 
    modifications to the SG internal structures, thereby limiting to a 
    small value, the maximum displacement of the TSPs under accident 
    conditions. The proposed structural modifications consist of expanding 
    a limited number of SG tubes only on the hot leg side of the TSP, at 
    each of the intersections of the tubes with the TSPs. The purpose of 
    this approach would be to greatly reduce the probability of SG tube 
    burst under postulated accident conditions by several orders of 
    magnitude. There would be a negligible impact on the primary-to-
    secondary SG tube leakage under accident conditions.
        While the voltage-based repair criteria for ODSCC flaws are 
    applicable only to Byron 1 and Braidwood 1, the pending request for 
    license amendments involves all four units in that both stations have a 
    common set of TSs. Date of publication of individual notice in Federal 
    Register: September 27, 1995 (60 FR 49963)
        Expiration date of individual notice: October 27, 1995
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Grundy County, Illinois
    
        Date of amendment request: September 1, 1995
        Description of amendment request: The proposed amendment would 
    upgrade the Dresden TS to the standard Technical Specifications (STS) 
    contained in NUREG-0123. The Technical Specification Upgrade Program 
    (TSUP) is not a complete adaption of the STS. The TS upgrade focuses on 
    (1) integrating additional information such as equipment operability 
    requirements during shutdown conditions, (2) clarifying requirements 
    such as limiting conditions for operation and action statements 
    utilizing STS terminology, (3) deleting superseded requirements and 
    modifications to the TS based on the licensee's responses to Generic 
    Letters (GL), and (4) relocating specific items to more appropriate TS 
    locations. The September 1, 1995, application proposed to upgrade only 
    Section 6.0 (Administrative Controls) of the Dresden TS.Date of 
    publication of individual notice in Federal Register: September 20, 
    1995 (60 FR 48728)
        Expiration date of individual notice: October 20, 1995
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: September 13, 1995
        Brief description of amendment request: The proposed amendments 
    would revise the Administrative Controls section and the Bases section 
    of the Beaver Valley Power Station, Unit Nos. 1 and 2 (BVPS-1 and BVPS-
    2), technical specifications to be consistent with the requirements of 
    the Offsite Dose Calculation Manual (ODCM). The ODCM was recently 
    updated to reflect the radioactive liquid and gaseous effluent release 
    limits and the liquid holdup tank activity limit of BVPS-1 License 
    Amendment No. 188 and BVPS-2 License Amendment No. 70 which were issued 
    June 12, 1995.Date of publication of individual notice in Federal 
    Register: September 22, 1995 (60 FR 49292)
        Expiration date of individual notice: October 23, 1995
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001
    
    [[Page 52938]]
    
    
    PECO Energy Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Docket No. 50-278, Peach Bottom Atomic Power Station, Unit 
    No. 3, York County, Pennsylvania
    
        Date of amendment request: September 1, 1995
        Brief description of amendment request: The proposed amendment 
    would delete License Condition 2.C.(5) from Facility Operating License 
    DPR-56 which restricts power levels to no less than seventy percent in 
    the coastdown condition.
        Date of publication of individual notice in Federal Register: 
    September 19, 1995 (60 FR 48530)
        Expiration date of individual notice: October 18, 1995
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: December 7, 1994, as 
    supplemented by letter dated August 1, 1995.
        Brief description of amendments: The amendments change Note 5 to 
    Table 4.3-1 of Technical Specification 3/4.3.1 to allow verification of 
    the shape-annealing matrix elements used in the core protection 
    calculators. This provides the option of using generic shape-annealing 
    matrix elements in the core protection calculators. Presently, cycle-
    specific shape-annealing elements are determined during startup testing 
    after each core reload. Use of a generic shape-annealing matrix 
    eliminates several hours of critical path work during startup after a 
    refueling outage.
        Date of issuance: September 20, 1995
        Effective date: September 20, 1995
        Amendment Nos.: Unit 1 - Amendment No. 100; Unit 2 - Amendment No. 
    88; Unit 3 - Amendment No. 71
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    495). The August 1, 1995, supplemental letter provided clarifying 
    information and did not change the original no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated September 20, 
    1995.No significant hazards consideration comments received: No
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
         Date of application for amendments: March 26, 1993, as 
    supplemented May 15, 1995
        Brief description of amendments: These amendments upgrade the 
    current custom Technical Specifications (TS) for Dresden and Quad 
    Cities to the Standard Technical Specifications contained in NUREG-
    0123, ``Standard Technical Specification General Electric Plants BWR/
    4.'' These amendments upgrade only Section 3/4.9 (Electrical Power 
    Systems). These amendments include the relocation of some TS 
    requirements to licensee-controlled documents.
        Date of issuance: September 18, 1995
        Effective date: Immediately, to be implemented no later than 
    December 31, 1995, for Dresden Nuclear Power Station and June 30, 1996, 
    for Quad Cities Nuclear Power Station.
        Amendment Nos.: 138, 132, 160, 156
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 19, 1994 (59 FR 
    2864) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 18, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois, 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: December 8, 1992, as 
    supplemented September 10, 1993, and May 17, 1995.
        Brief description of amendments: This application upgrades the 
    current custom Technical Specifications (TS) for Dresden and Quad 
    Cities to the Standard Technical Specifications (STS) contained in 
    NUREG-0123, ``Standard Technical Specification General Electric Plants 
    BWR/4.'' This application upgrades only Section 3/4.1 (Reactor 
    Protection System). Date of issuance: 
    
    [[Page 52939]]
    September 20, 1995Effective date: Immediately, to be implemented no 
    later than December 31, 1995, for Dresden Station and June 30, 1996, 
    for Quad Cities Station.
        Amendment Nos.: 139, 133, 161, and 157
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29872) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 20, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: September 17, 1993, as 
    supplemented June 30, 1995.
        Brief description of amendments: This application upgrades the 
    current custom Technical Specifications (TS) for Dresden and Quad 
    Cities to the Standard Technical Specifications (STS) contained in 
    NUREG-0123, ``Standard Technical Specification General Electric Plants 
    BWR/4.'' This application upgrades only Section 3/4.6.
        Date of issuance: September 21, 1995
        Effective date: Immediately, to be implemented no later than 
    December 31, 1995, for Dresden Station and June 30, 1996, for Quad 
    Cities Station.
        Amendment Nos.: 140, 134, 162, and 158
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37087) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 21, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: April 11, 1995
        Brief description of amendments: The amendments allow a one-time 
    extension of specific LaSalle, Units 1 and 2, 18-month Technical 
    Specification Surveillance Requirements to allow surveillance testing 
    to coincide with the LaSalle, Unit 1, seventh refueling outage (L1R07). 
    The shutdown for L1R07 has been rescheduled from September 1995 until 
    early 1996. The proposed extensions apply to calibrations and 
    functional testing of isolation actuation instrumentation, emergency 
    core cooling system actuation instrumentation, and recirculation pump 
    trip actuation instrumentation; leakage testing of reactor coolant 
    system isolation valves; inspection of fire-rated seals; functional 
    testing of mechanical snubbers; inspections of emergency diesel 
    generators; and testing of batteries, battery chargers, and other 
    electrical components.
        Date of issuance: September 27, 1995
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.:  106 and 92
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Facility Operating Licenses.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35066) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 27, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: June 17, 1993, as supplemented 
    July 5, 1995
        Brief description of amendments: The amendments revise Technical 
    Specification Section 5.3.1 ``Fuel Assemblies'' in accordance with 
    Generic Letter 90-02, Supplement 1, ``Alternative Requirements For Fuel 
    Assemblies in The Design Features Section of Technical 
    Specifications.''
        Date of issuance: September 18, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance
        Amendment Nos.: 135 and 129
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 21, 1993 (58 FR 
    39048) and ReNoticed August 16, 1995 (60 FR 42601) The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated September 18, 1995. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley 
    Power Station, Unit No. 1, Shippingport, Pennsylvania
    
        Date of application for amendment: July 11, 1995
        Brief description of amendment: This amendment revised the required 
    area of the reactor coolant system overpressure protection system vent 
    from 3.14 square inches to 2.07 square inches which is equal to the 
    relief area of a single power-operated relief valve.
        Date of issuance: September 26, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 193
        Facility Operating License No. DPR-66. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42603) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 26, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    PowerStation, Unit 2, Shippingport, Pennsylvania
    
        Date of application for amendment: July 24, 1995
        Brief description of amendment: This amendment revises TS 3/4.4.11, 
    ``Relief Valves,'' and associated Bases to make Unit 2 TS 3/4.4.11 
    consistent with Unit 1 TS 3/4.4.11 which was revised by Unit 1 License 
    Amendment No. 187 issued on May 15, 1995. The amendment generally 
    reflects the guidance provided in NRC Generic Letter 90-06 and in the 
    NRC's Improved Standard Technical Specifications (NUREG-1431).
        Date of issuance: September 18, 1995
    
    [[Page 52940]]
    
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 76
        Facility Operating License No. NPF-73: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42604) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 18, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: March 17, 1995
        Brief description of amendment: The amendment revises requirements 
    associated with the frequency of containment post-entry visual 
    inspections.
        Date of issuance: September 15, 1995
        Effective date: September 15, 1995
        Amendment No.: 162
        Facility Operating License No. NPF-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37089) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 15, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: October 27, 1993
        Brief description of amendment: The amendment relocated reactor 
    incore detector requirements from the TSs to the safety analysis 
    report.
        Date of issuance: September 15, 1995
        Effective date: September 15, 1995
        Amendment No.: 163
        Facility Operating License No. NPF-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64606) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 15, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: March 17, 1995
        Brief description of amendment: The amendment transfers 
    requirements for cycle specific core operating limits from the 
    Technical Specifications to the Core Operating Limits Report. 
    Additionally, a reference to a statistical methodology for determining 
    uncertainties is being changed to reference a methodology that was 
    recently approved by the NRC.
        Date of issuance: September 19, 1995
        Effective date: September 19, 1995
        Amendment No.: 164
        Facility Operating License No. NPF-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37088) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 19, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: April 4, 1995, as supplemented 
    August 25, 1995
        Brief description of amendment: The amendment provides a one-time 
    extension of the reactor coolant pump flywheel inservice inspection.
        Date of issuance: September 22, 1995
        Effective date: September 22, 1995
        Amendment No.: 165
        Facility Operating License No. NPF-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35069) The August 25, 1995, submittal did not change the original no 
    significant hazards consideration determination.The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated September 22, 1995. No significant hazards consideration comments 
    received: No
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: May 19, 1995 as supplemented 
    July 21, 1995.
        Brief description of amendment: The amendment revises the 
    specifications to permit the containment personnel airlock doors to 
    remain open during fuel handling.
        Date of issuance: September 28, 1995
        Effective date: September 28, 1995
        Amendment No.: 166
        Facility Operating License No. NPF-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39437) The July 22, 1995, supplement provided clarifying information 
    and did not change the original no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 28, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: April 4, 1995, as 
    supplementedSeptember 28, 1995
        Brief description of amendment: The amendment removes the 
    requirement to maintain water level 23 feet above irradiated fuel 
    assemblies in the reactor while latching and unlatching control element 
    assemblies.
        Date of issuance: September 28, 1995
        Effective date: September 28, 1995
        Amendment No.: 167
        Facility Operating License No. NPF-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42604) The September 28, 1995, submittal provided clarifying 
    information and did not change the original no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated September 28, 1995. 
    No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    [[Page 52941]]
    
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: June 22, 1994, as supplemented by 
    letters dated June 28, 1995 and August 22, 1995
        Brief description of amendment: The amendment changes the Appendix 
    A TSs by increasing the control room radiation monitor setpoint (CRRMS) 
    to a fixed value of 5.45E-6 micro curies per cubic centimeters instead 
    of being set at two times the background.
        Date of issuance: September 27, 1995
        Effective date: Septembe 27, 1995
        Amendment No.: 114
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39586) The June 28, 1995 and August 22, 1995, letters provided 
    clarifying information that did not change the originial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated September 27, 1995. No significant hazards consideration comments 
    received: No
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: August 11, 1995
        Brief description of amendment: The amendment removes the Technical 
    Specifications for the Makeup, Purification, and Chemical Addition 
    Systems from the Technical Specifications (Section 3.2) and relocates 
    the pertinent design information, including tank volume and boron 
    concentrations, to the TMI-1 Updated Final Safety Analysis Report.
        Date of issuance: September 19, 1995
        Effective date: September 19, 1995
        Amendment No.: 196
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 18, 1995 (60 FR 
    43172) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated September 19, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location:  Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: June 9, 1995
        Brief description of amendment: The amendment modifies Technical 
    Specification 4.1, ``Site Location,'' to incorporate a description of 
    the exclusion area boundary. The change is necessary to ensure the 
    content of the technical specifications conform to Section 182 of the 
    Atomic Energy Act of 1954.
        Date of issuance: September 14, 1995
        Effective date:  September 14, 1995
        Amendment No.: 101
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37093) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 14, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: July 21, 1995
        Brief description of amendment: The amendment revised Technical 
    Specifications Section 6.0 (Administrative Controls) to replace the 
    title-specific list of members on the Plant Operating Review Committee 
    (PORC) with a more general statement of membership requirements. The 
    scope of disciplines represented on the PORC was also expanded to 
    include nuclear licensing and quality assurance. The amendment also 
    changed the title ``Resident Manager'' to ``Site Executive Officer.'' 
    This title change was an administrative change that did not affect the 
    reporting relationship, authority, or responsibility of the position.
        Date of issuance: September 20, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 163
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42606) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 20, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: April 25, 1994
        Brief description of amendment: This amendment revises TS Section 
    3.8.1.1, ``A.C. Sources - Operating,'' TS Section 3.8.1.2, ``A.C. 
    Sources - Shutdown,'' and associated Bases, to increase the required 
    quantity of fuel in the Emergency Diesel Generator Fuel Oil Day Tanks 
    from 200 to 360 gallons.
        Date of issuance: September 15, 1995
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days.
        Amendment No.: 79
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29632)The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 15, 1995. No significant hazards 
    consideration comments received: No
        Local Public Document Room location:  Pennsville Public Library, 
    190 S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: January 20, 1995
        Brief description of amendment: This amendment changes Technical 
    Specification (TS) 4.1.3.1.2.b, ``Control Rods - Surveillance 
    Requirement'' to change the required action to be taken when a control 
    rod becomes immovable due to excessive friction from ``at least once 
    per'' 24 hours to ``within'' 24 hours.
        Date of issuance: September 20, 1995
        Effective date: As of its date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 80
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications. 
    
    [[Page 52942]]
    
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39452) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 20, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: January 11, 1995
        Brief description of amendment: This amendment changes Technical 
    Specification (TS) 3/4.3.8, ``Turbine Overspeed Protection System,'' 
    removing these requirements from the TS and relocating the Bases to the 
    Hope Creek Updated Final Safety Analysis Report (UFSAR) and the 
    Surveillance Requirements to the applicable surveillance procedures. 
    The Limiting Conditions for Operation (LCOs) are eliminated.
        Date of issuance: September 25, 1995
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days.
        Amendment No.: 81
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39451). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 25, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: September 29, 1994
        Brief description of amendment: This amendment changes Technical 
    Specification (TS) Sections 3/4.3.7.2, ``Seismic Monitoring 
    Instrumentation,'' and 3/4.3.7.3, ``Meteorological Instrumentation,'' 
    to remove the requirements from the TS and relocate the appropriate 
    descriptive information and testing requirements to the Hope Creek 
    Updated Final Safety Analysis Report.
        Date of issuance: September 25, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 82
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39449). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 25, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: September 20, 1994
        Brief description of amendments: The amendments change the Channel 
    Functional Test surveillance frequency for the Manual Reactor Trip 
    Switches and Reactor Trip Breakers (RTB) and relocate the RTB 
    maintenance requirements from the Technical Specifications to the Salem 
    Updated Final Safety Analysis Report.
        Date of issuance: September 18, 1995
        Effective date: Both units, as of the date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 176 and 157
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55890 The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 18, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: January 21, 1994, as 
    supplemented June 28 and September 13, 1994, and April 4, 1995.
        Brief description of amendments: Revised Technical Specifications 
    3.8.2.3, ``125-Volt D.C. DISTRIBUTION - OPERATING.''
        Date of issuance: September 19, 1995
        Effective date: Both units, as of the day of issuance and shall be 
    implemented within 60 days.
        Amendment Nos.: 177 and 158
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (58 FR 
    22012) The June 28 and September 13, 1994, and April 4, 1995 letters 
    provided clarifying information that did not change the scope of the 
    January 21, 1994 application and initial proposed no significant 
    hazards consideration determination, nor go beyond the scope of the 
    Federal Register notice. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated September 19, 
    1995. No significant hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: June 19, 1995, as supplemented 
    on August 21, 1995.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to change the required test frequency for the reactor 
    building spray nozzle flow test from once per five years to once per 
    ten years.
        Date of issuance: September 18, 1995
        Effective date: September 18, 1995
        Amendment No.: 127
        Facility Operating License No. NPF-12: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37100). The August 21, 1995 letter provided supplemental information 
    that did not change the initial proposed no significant hazards 
    consideration. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 18, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: July 28, 1995
    
    [[Page 52943]]
    
        Brief description of amendment: The amendment revises the Technical 
    Specifications to exclude the requirement to perform the slave relay 
    test of the 36-inch containment purge supply and exhaust valves on a 
    quarterly basis while the plant is in Modes 1, 2, 3, or 4.
        Date of issuance: September 18, 1995
        Effective date: September 18, 1995
        Amendment No.: 128
        Facility Operating License No. NPF-12. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42608) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 18, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: June 19, 1995, as supplemented 
    on August 21, 1995.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to change the required test frequency for the reactor 
    building spray nozzle flow test from once per five years to once per 
    ten years.
        Date of issuance: September 18, 1995
        Effective date: September 18, 1995
        Amendment No.: 129
        Facility Operating License No. NPF-12. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37100). The August 21, 1995 letter provided supplemental information 
    that did not change the initial proposed no significant hazards 
    consideration. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 18, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: April 3, 1995
        Brief description of amendment: The amendment revised the Technical 
    Specifications (TS) to relocate radiological effluent and radiological 
    environmental monitoring TS to the Offsite Dose Calculation Manual or 
    to the Process Control Program. Programmatic controls for radioactive 
    effluent and radiological environmental monitoring were included in TS 
    6.8.4.
        Date of issuance: September 15, 1995
        Effective date: September 15, 1995
        Amendment No.: 72
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24921) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 15, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: June 1, 1995
        Brief description of amendment: The amendment revised the Technical 
    Specifications to make them more restrictive regarding control rod 
    drive scram time testing. CRD scram time testing would be required 
    following maintenance prior to considering the CRD operable, and could 
    be performed at any reactor pressure. Additional testing would be 
    required when reactor coolant pressure is greater than or equal to 950 
    psig and prior to 40 percent rated thermal power.
        Date of issuance: September 26, 1995
        Effective date: September 26, 1995
        Amendment No. 73
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39452) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 26, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: January 14, 1992, as 
    supplemented by letters dated February 10, 1995, and August 16, 1995.
        Brief description of amendment: The amendment revises technical 
    specification surveillance requirements regarding demonstration of jet 
    pump operability and corrects several administrative discrepancies.
        Date of issuance: September 18, 1995
        Effective date: September 18, 1995, to be implemented within 30 
    days of issuance
        Amendment No.: 141
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 27, 1992 (57 FR 
    22272) and March 29, 1995 (60 FR 16204). The August 16, 1995, 
    supplemental letter provided additional clarifying information and did 
    not change the initial no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 18, 1995.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Dated at Rockville, Maryland, this 3rd day of October 1995.
        For the Nuclear Regulatory Commission
    Elinor G. Adensam,
    Deputy Director, Division of Reactor Projects - III/IV, Office of 
    Nuclear Reactor Regulation
    [Doc. 95-25006 Filed 10-10-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Effective Date:
9/20/1995
Published:
10/11/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X95-11011
Dates:
September 20, 1995
Pages:
52926-52943 (18 pages)
PDF File:
x95-11011.pdf