X94-11012. Biweekly Notice  

  • [Federal Register Volume 59, Number 196 (Wednesday, October 12, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-11012]
    
    
    [[Page Unknown]]
    
    [Federal Register: October 12, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
     
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from September 19, 1994, through September 29, 
    1994. The last biweekly notice was published on September 28, 1994 (59 
    FR 49425).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By November 14, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: August 19, 1994
        Description of amendment request: The proposed amendment will move 
    the current procedural details of the radiological effluent Technical 
    Specifications (TS) programmatic controls for radioactive effluents, 
    radiological environmental monitoring and solid radioactive wastes from 
    the Administrative Controls Section of the TS to the Offsite Dose 
    Calculation Manual (ODCM) or the Process Control Program (PCP), as 
    appropriate, in accordance with the guidance of Generic Letter 89-01. 
    This amendment will also incorporate changes to the reporting 
    requirements for the Effluent Release Reports, in accordance with 10 
    CFR 50.36; incorporate references to the new 10 CFR Part 20; and revise 
    the terminology for the gaseous effluent release rate limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Transferring the procedural details from the TS to the ODCM and 
    PCP and their replacement with programmatic controls have no impact 
    on plant operation or safety. No safety-related equipment, safety 
    function, or plant operation will be altered as a result of this 
    proposed change. The changes are unrelated to the initiation and 
    mitigation of accidents and equipment malfunctions addressed in the 
    Final Safety Analysis Report.
        The proposed revisions to the reporting requirements for 
    Effluent Release Reports, the gaseous effluent release rate limit 
    and the relocation of the old 10 CFR 20.106 requirements to the new 
    10 CFR 20.1302 have no impact on plant systems, plant operations or 
    accident precursors. The changes to the Effluent Report requirements 
    and the updated reference to 10 CFR 20.1302 are administrative in 
    nature. The change to the gaseous effluent release limit is also 
    administrative in nature in that it will allow the continued 
    operation of the facility with the same release rate limits as are 
    currently implemented by the Technical Specifications.
        Therefore, there would be no increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Transferring the procedural details from the TS to the ODCM and 
    PCP and their replacement with programmatic controls have no impact 
    on plant operation or safety. No safety-related equipment, safety 
    function, or plant operation will be altered as a result of this 
    proposed change. No changes to plant components or structures are 
    introduced which could create new accidents or malfunctions not 
    previously evaluated.
        The proposed revisions to the reporting requirements for 
    effluent Release Reports, the gaseous effluent release rate limit 
    and the relocation of the old 10 CFR 20.106 requirements to the new 
    10 CFR 20.1302 have no impact on plant systems, plant operations or 
    accident precursors. The changes to the Effluent Report requirements 
    and the updated reference to 10 CFR 20.1302 are administrative in 
    nature. The change to the gaseous effluent release limits is also 
    administrative in nature in that it will allow the continued 
    operation of the facility with the same release rate limits as are 
    currently implemented by the Technical Specifications.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident
        previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The procedural details of the current RETS will be transferred 
    to the ODCM and PCP and replaced with programmatic controls 
    consistent with regulatory requirements, including controls on 
    revisions to the ODCM and PCP. Thus, no requirements or controls 
    will be reduced.
        The changes to the Effluent Report requirements and the updated 
    reference to 10 CFR 20.1302 are administrative in nature and 
    therefore have no effect on the margin of safety. The proposed 
    revisions to the gaseous effluent release limits will maintain the 
    release rate limits at the same level as currently implemented by 
    the Technical Specifications. Therefore, there will be no change in 
    the types and amounts of effluents that will be released, nor will 
    there be an increase in individual or cumulative radiation exposures 
    to any member of the public.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: David B. Matthews
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: September 19, 1994
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications by reducing the frequency for 
    testing the containment spray system spray nozzles.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability of occurrence or consequences of any accident 
    previously evaluated.
        The relaxation of surveillance frequency will not affect any of 
    the initiators or precursors of any accident previously evaluated. 
    Performance of CS spray nozzle testing on a ten year basis rather 
    than on a five year basis will not increase the likelihood that a 
    transient initiating event will occur because transients are 
    initiated by external events, equipment malfunction, and/or 
    catastrophic system failure. There are no failure mechanisms or 
    modes for the CS system or spray nozzles that could initiate a 
    transient since the CS system is passive except during a Loss of 
    Coolant Accident (LOCA). Upon receipt of a Containment Spray signal 
    (Containment High-High Pressure coincident with a Safety Injection 
    Signal), the CS pumps automatically start and valves align to 
    provide spray flow through the CS risers, ring headers, and out the 
    spray nozzles. Periodic testing requirements for the CS pumps and 
    valves (the active components of the system) are unaffected by the 
    proposed changes. Industry experience and previous test experience 
    at Zion Station supports the conclusion that functional checks of 
    the spray nozzles on a ten year basis is adequate to detect 
    degradation or blockage of the spray nozzles.
        The proposed typographical and administrative changes do not 
    affect the operability or surveillance requirements given in 
    Technical Specifications. They will only improve consistency of 
    existing terminology and format of Technical Specifications and will 
    remove temporarily imposed Bases that are no longer applicable.
        Based on the fact that reliability of the system will not be 
    affected and transient precursors and initiators are not affected by 
    operation in accordance with the proposed changes, the probability 
    of occurrence of accidents previously evaluated will not 
    significantly increase.
        The proposed change in surveillance frequency will not affect 
    the ability of the CS system to function as designed during the 
    accidents considered in the Safety Analyses. Periodic testing 
    requirements for the CS pumps and valves (the active components of 
    the system) are unaffected by the proposed changes. Industry 
    experience and previous test experience at Zion Station supports the 
    conclusion that functional checks of the spray nozzles on a ten year 
    basis is adequate to detect degradation or blockage of the spray 
    nozzles. Given the proposed changes, the CS system will maintain the 
    ability to reduce containment pressure, remove heat from 
    containment, and remove iodine from the containment atmosphere 
    during the design basis LOCA. As a result, peak containment pressure 
    will be maintained below design pressure and the off-site release 
    due to the postulated accident will remain as described in the 
    Safety Analyses. Therefore, based on the previous discussion, the 
    proposed changes do not involve a significant increase in 
    consequences of any accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        The proposed changes to the Technical Specifications do not 
    involve the addition of any new or different types of safety related 
    equipment, nor does it involve the operation of equipment required 
    for safety operation of the facility in a manner different from 
    those addressed in the safety analyses. No safety related equipment 
    or function will be altered as a result of the proposed changes. 
    Also, changes to the procedures governing normal plant operation and 
    recovery from an accident are not necessitated by the proposed 
    Technical Specification changes.
        The proposed typographical and administrative changes do not 
    affect the operability or surveillance requirements given in 
    Technical Specifications. They will only improve consistency of 
    existing terminology and format of Technical Specifications and will 
    remove Bases that are no longer applicable.
        Since no new failure modes or mechanisms are added by the 
    proposed changes, the possibility or a new or different kind of 
    accident is not created.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        Plant safety margins are established through LCOs, limiting 
    safety system settings, and safety limits specified in the Technical 
    Specifications. There will be no changes to either the physical 
    design of the plant or to any of these settings and limits as a 
    result of relaxing the surveillance frequency of CS nozzle checks 
    from five years to ten years. Testing on a ten year basis is 
    adequate to detect spray nozzle degradation or blockage since the 
    system piping and spray nozzles are constructed of corrosion 
    resistant Type 304 stainless steel and since the system is normally 
    passive (i.e. spray risers and spray rings are empty with no flow 
    except during an accident). This conclusion was also provided in 
    NUREG-1366 and Generic Letter 93-05 which recommended revising the 
    surveillance frequency as proposed.
        The proposed typographical and administrative changes do not 
    affect the operability or surveillance requirements given in 
    Technical Specifications. They will only improve consistency of 
    existing terminology and format of Technical Specifications and will 
    remove Bases that are no longer applicable.
        Based on the above discussion, the ability to safely shut down 
    the operating unit and mitigate the consequences of all accidents 
    previously evaluated will be maintained. Therefore, the margin of 
    safety is not significantly affected.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: Robert A. Capra
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: August 25, 1994
        Description of amendment request: The requested amendments modify 
    the trip setpoint and allowable value for the 4 kilo-volt (KV) 
    electrical bus degraded grid undervoltage relay and the allowable value 
    for the loss of offsite power relay in response to an issue identified 
    in the licensee's Self-Initiated Technical Audit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1
        The requested amendments will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The amendments will not affect either the probability or 
    the consequences of an accident, since no physical changes to the 
    plant are being proposed. The amendments merely change the existing 
    technical specification settings for the above relays to more 
    conservative values. Current field settings for these relays are 
    already at these more conservative values. No changes to the manner 
    in which the plant is operated are being proposed.
        Criterion 2
        The requested amendments will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. As stated above, no actual changes to the physical plant 
    are being proposed. No effect on plant operation will occur, 
    therefore the possibility of new accident types is not created.
        Criterion 3
        The requested amendments will not involve a significant 
    reduction in a margin of safety. Plant safety margins will be 
    unaffected, since no changes to the plant are being made. The 
    proposed technical specification values are more conservative and 
    are intended to make the technical specifications correspond with 
    the actual plant relay settings.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: August 25, 1994
        Description of amendment request: The amendments would change the 
    frequency for conducting the surveillance test required by TS 4.7.1.2.1 
    for the auxiliary feedwater pumps from once per 31 days to at least 
    once per 92 days and would add a footnote which clarifies that testing 
    is not required to be performed until system heatup has progressed to a 
    pressure (600 psig) that will support conduct of the test. The change 
    in the surveillance frequency has been evaluated and approved by the 
    NRC staff as discussed in Section 9.1 of NUREG-1366, ``Improvements to 
    Technical Specifications Surveillance Requirements.'' The change is 
    based on the finding in NUREG-1366 that an analysis of AFW pump 
    failures indicates that a monthly surveillance test interval may be 
    contributing to AFW pump unavailability through failures and equipment 
    degradation and, therefore, AFW pump availability is increased by 
    quarterly testing on a staggered basis. Generic Letter 93-05, ``Line-
    Item Technical Specification Improvements to Reduce Surveillance 
    Requirements for Testing During Power Operation,'' provided the sample 
    TS for this change. The change is accomplished by dividing TS 
    4.7.1.2.1a into two parts. The new 4.7.1.2.1a maintains the previous 
    31-day testing frequency for the AFW valves while the new 4.7.1.2.1b 
    inserts a new frequency of once per 92 days for the AFW pump tests. 
    Also, an obsolete footnote is deleted. The new footnote discussed above 
    is consistent with NUREG-1431, ``Standard Technical Specifications for 
    Westinghouse Plants.'' Appropriate changes to the Bases for the TS have 
    also been proposed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The requested amendments decrease from monthly to quarterly the 
    frequency at which the motor-driven and turbine-driven AFW pumps 
    must be demonstrated operable as specified in TS 4.7.1.2.1. They 
    also incorporate a note of clarification from the new Westinghouse 
    STS into the existing Catawba specifications concerning when the 
    pump head or discharge pressure versus flow verification for the 
    turbine-driven pump is required to be performed.
        Criterion 1
        The requested amendments will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Decreasing the frequency of AFW pump testing as specified 
    in TS from monthly to quarterly will have no impact upon the 
    probability of any accident, since the AFW pumps are not accident 
    initiating equipment. Also, since Catawba's AFW pump performance 
    history supports making the proposed change, system response 
    following an accident will not be adversely affected. Therefore, the 
    requested amendments will not result in increased accident 
    consequences. Deletion of the obsolete footnotes as indicated in the 
    Catawba technical specification markups is purely an administrative 
    change, and therefore will have no impact upon either the 
    probability or consequences of any accident. Incorporating the new 
    STS note will only serve to clarify when the turbine-driven pump is 
    required to be tested and will not have any impact upon either the 
    probability or consequences of any accident. The pump will still be 
    tested as before and its acceptance criteria will be unaffected.
        Criterion 2
        The requested amendments will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. As stated above, the AFW pumps are not accident 
    initiating equipment. No new failure modes can be created from an 
    accident standpoint. The plant will not be operated in a different 
    manner. Deletion of the Catawba obsolete footnotes has no bearing on 
    any accident initiating mechanisms. Incorporating the clarifying 
    note from the new STS will not result in any new acident sequences, 
    since plant operation will be unaffected.
        Criterion 3
        The requested amendments will not involve a significant 
    reduction in a margin of safety. Plant safety margins will be 
    unaffected by the proposed changes. The AFW pumps will still be 
    capable of fulfilling their required safety function, since plant 
    operating experience supports the proposed change. The availability 
    of the AFW pumps will be increased as a result of the proposed 
    amendments because they will not have to be made unavailable for 
    testing as frequently. Finally, the proposed amendments are 
    consistent with the NRC position and guidance set forth in NUREG-
    1366 and Generic Letter 93-05. Deletion of the Catawba obsolete 
    footnotes will not result in any impact to plant safety margins. 
    Incorporating the note from the new STS will not impact any safety 
    margins.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: September 1, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3.2.2, ``Minimum Reactor Vessel 
    Temperature for Pressurization,'' and the associated Bases. 
    Specifically, the proposed amendment replaces existing TS Figures 
    3.2.2.a,b,c,d, and e and associated TS Tables 3.2.2.a,b,c,d, and e, 
    that define the limits for minimum reactor vessel temperature for 
    pressurization and account for neutron damage at exposures up to 18 
    effective full power years (EFPY), with new figures and tables that are 
    applicable for up to 18 EFPY. The licensee stated that the new 
    pressure-temperature (P-T) limits were developed based on a plant-
    specific Charpy shift model for Nine Mile Point Nuclear Station Unit 
    No. 1 which is consistent with and meets the requirements of Regulatory 
    Guide 1.99, Revision 2, ``Radiation Embrittlement of Reactor Vessel 
    Materials.'' The new P-T limits were calculated in accordance with 10 
    CFR Part 50, Appendix G, and with the requirements specified in 
    Appendix G to Section III of the American Society of Mechnical 
    Engineers Boiler and Pressure Vessel Code (ASME Code).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 1 [NMP1], in accordance 
    with the proposed amendment, will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Components of the reactor primary coolant system are operated so 
    that no substantial mechanical or thermal loading is applied unless 
    the reactor pressure vessel (RPV) materials are at a temperature 
    well above the reference nil-ductility temperature (RTNDT) of 
    the limiting RPV material. Protection against brittle fracture is 
    further ensured by postulating a defect with a depth 1/4 of the RPV 
    wall thickness and a length 1-1/2 times the wall thickness, and 
    calculating the allowable pressure loading as a function of 
    temperature using linear elastic fracture mechanics. Safety factors 
    are applied to the allowable loading determination and lower bound 
    fracture toughness properties are used to represent the material 
    behavior. The net effect of the 10 CFR [Part] 50, Appendix G and the 
    ASME Section III, Appendix G P-T curve calculative procedures is to 
    produce very conservative P-T curves. These procedures have been 
    applied in the calculation of the proposed P-T limits.
        Neutron damage during plant operation is accounted for in the 
    allowable pressure loading by calculating an adjusted reference nil-
    ductility temperature (ARTNDT). Regulatory Guide 1.99, Revision 
    2, defines the ARTNDT as the sum of the reference nil-ductility 
    temperature (RTNDT) plus the shift in the reference nil-
    ductility temperature caused by irradiation ([delta]RTNDT), 
    plus a margin. The proposed amendment replaces Equation (2) in 
    Regulatory Position 2.1 with an accurate plant-specific model. The 
    ARTNDT margin is the same as for earlier P-T curve 
    calculations. Operation of NMP1 in accordance with the proposed P-T 
    operating limits will preclude brittle failure of the RPV materials. 
    Safety margins for brittle fracture are in accordance with those 
    specified in 10 CFR [Part] 50, Appendix G and Appendix G to Section 
    III of the ASME Code. Therefore, the proposed amendment will not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed amendment incorporates P-T operating limits based 
    on previously established calculative procedures described in 10 CFR 
    [Part] 50, Appendix G, Appendix G to Section III of the ASME Code, 
    and Regulatory Guide 1.99, Revision 2. The proposed changes to the 
    P-T operating limits are based on analyses of the irradiated 
    limiting plate material for Nine Mile Point Unit 1. The proposed 
    changes do not modify any plant equipment nor do they create any 
    potential initiating events that would create any new or different 
    kind of accident. Operation in accordance with the proposed P-T 
    operating limits will preclude brittle failure of the reactor vessel 
    material, since safety margins specified in 10 CFR [Part] 50, 
    Appendix G and Appendix G to Section III of the ASME Code will be 
    maintained. Therefore, the proposed P-T limits will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    amendment, will not involve a significant reduction in a margin of 
    safety.
        Operation in accordance with the proposed P-T operating limits 
    will preclude brittle failure of the reactor pressure vessel since 
    safety margins in 10 CFR [Part] 50, Appendix G and Appendix G to 
    Section III of the ASME Code will be maintained. The plant-specific 
    limiting material [delta]RTNDT has been reduced as compared 
    with the overly conservative [delta]RTNDT used in previous P-T 
    curve calculations as a result of the more accurate representation 
    of the Nine Mile Point Unit 1 RPV plate behavior as a function of 
    neutron exposure. However, the [delta]RTNDT is intended to be 
    an accurate representation of the Charpy shift (indexed at 30 ft-lbs 
    of absorbed energy) as a function of fluence. Since the ASME Section 
    III, Appendix G safety factors have been maintained and the 
    Regulatory Guide 1.99, Revision 2, margin term specified in 
    Regulatory Position 2.1 has been applied in the same manner as in 
    earlier P-T curve calculations, no significant reduction in the 
    margin of safety has resulted from the use of a plant-specific 
    [delta]RTNDT model. Therefore, the proposed amendment will not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Michael J. Case
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-
    323,Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment request: August 17, 1994 (Reference LAR 94-06)
        Description of amendment request: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant (DCPP) Unit Nos. 1 and 2 to change TS 3/4.1.2.5, ``Borated 
    Water Sources - Shutdown,'' TS 3/4.1.2.6, ``Borated Water Sources - 
    Operating,'' and TS 3/4.5.5, ``Emergency Core Cooling Systems - 
    Refueling Water Storage Tank.'' The changes delete the minimum 
    refueling water storage tank (RWST) solution temperature and increase 
    the allowed outage time (AOT) of the RWST for adjustment of boron 
    concentration from 1 hour to 8 hours. Specifically, the minimum RWST 
    temperature requirement of TS 3.1.2.5b(3), TS 4.1.2.5b, and TS 4.5.5b 
    would be deleted. TS 3/4.1.2.6 would be revised as follows: (1) TS 
    3.1.2.6b, Action Statement b., and TS 4.1.2.6b, pertaining to the RWST, 
    would be deleted. (2) Editorial changes would be made to reflect the 
    deletion of the RWST requirements. TS 3/4.5.5 would be revised as 
    follows: the minimum RWST temperature requirement of TS 3.5.5c would be 
    deleted, and the action statement would be deleted and replaced with 
    two action statements. Action Statement a. would specify the 
    requirements when the RWST is inoperable due to boron concentration. 
    The action statement would also provide 8 hours to restore the boron 
    concentration to within the required limits. If boron concentration is 
    not restored within 8 hours, the action statement requires that the 
    unit be in hot standby within 6 hours and in cold shutdown within the 
    following 30 hours. Action Statement b. would specify the requirements 
    when the RWST is inoperable due to reasons other than boron 
    concentration. The associated Bases would also be appropriately 
    revised.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The increase in the RWST AOT does not alter the plant 
    configuration or operation. The potential for the RWST boron 
    concentration to be outside the TS limits is small because the RWST 
    and its contents are not involved with normal plant operation and 
    are not subject to process variations associated with plant 
    operation.
        The potential causes of boron concentration deviation have been 
    evaluated with the conclusion that any deviation in RWST boron 
    concentration would not be expected to increase significantly during 
    the proposed 7 hour AOT increase.
        The increase in the RWST AOT from 1 hour to 8 hours for reasons 
    directly related to boron concentration does not have a significant 
    effect on the accident analyses.
        The removal of the redundant statement of RWST requirements from 
    TS 3.1.2.6 is an administrative change with no impact on plant 
    operation.
        The removal of the minimum temperature limit for the RWST has no 
    effect on the plant configuration or operation. The removal of the 
    temperature limits does not affect any accident analyses since 
    evaluations have demonstrated that, due to the moderate climate at 
    DCPP, the RWST will not exceed the limits assumed in DCPP accident 
    analyses.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Increasing the RWST AOT from 1 hour to 8 hours for reasons 
    directly related to boron concentration does not require physical 
    alteration to any plant system and does not change the method by 
    which any safety-related system performs its function.
        The removal of the redundant statement of RWST requirements from 
    TS 3.1.2.6 is an administrative change that does not affect the 
    design and operation of the plant.
        Deletion of the RWST temperature has no impact on any accident 
    analysis due to the moderate climate at DCPP. Additionally, the 
    deletion of the temperature does not require any physical alteration 
    to the plant or change the method by which any safety-related system 
    performs its function.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        Increasing the RWST AOT for reasons directly related to boron 
    concentration does not affect any accident analysis assumptions, 
    initial conditions, or results. The margins of safety reflected in 
    the DCPP TS are not compromised by the 7 hour AOT increase. 
    Consequently, the proposed change does not have an effect on margin 
    of safety.
        The removal of the redundant statement of RWST requirements from 
    TS 3.1.2.6 is an administrative change that does not affect the 
    requirements for the RWST nor alter its function.
        The removal of the RWST temperature limits will not affect the 
    assumptions of any accident analysis because the moderate climate at 
    DCPP will prevent the temperature assumptions in the analyses from 
    being exceeded.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas & 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Theodore R. Quay
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-
    323,Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment request: August 17, 1994 (Reference LAR 94-07)
        Description of amendment request: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant Unit Nos. 1 and 2 to relocate TS 3/4.4.2.1, ``Safety Valves 
    - Shutdown,'' 3/4.4.7, ``Chemistry,'' 3/4.4.9.2, ``Pressurizer 
    (Temperature Limits),'' 3/4.4.10, ``Structural Integrity,'' and 3/
    4.4.11, ``Reactor Vessel Head Vents,'' in accordance with the 
    Commission's Final Policy Statement for relocation of current TS that 
    do not satisfy any of the screening criteria for retention. As part of 
    the relocation of TS 3/4.4.2.1, TS 3/4.4.2.2, ``Safety Valves - 
    Operating,'' would be revised to require that the pressurizer safety 
    valves be operable in Mode 4 with the reactor coolant system cold-leg 
    temperature greater than the low-temperature overpressure protection 
    system enable temperature, and TS 6.8, ``Procedures and Programs,'' 
    would be revised to include the reactor coolant pump flywheel 
    inspection program. The specific TS changes proposed are as follows:
        (1)
        Technical Specifications (TS) 3/4.4.2.1 ``Safety Valves - 
    Shutdown,'' 3/4.4.7, ``Chemistry,'' 3/4.4.9.2, ``Pressurizer 
    (Temperature Limits),'' 3/4.4.10, ``Structural Integrity,'' 3/4.4.11, 
    ``Reactor Vessel Head Vents,'' and TS 6.8, ``Procedures and Programs,'' 
    would be revised in accordance with the Commission's Final Policy 
    Statement on TS Improvements for Nuclear Power Reactors.
        (2)
        TS 3/4.4.2.2, ``Safety Valves - Operating,'' would be revised to 
    require that the pressurizer safety valves be operable in Mode 4 with 
    the reactor coolant system cold-leg temperature greater than the low- 
    temperature overpressure protection system enable temperature.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Do the changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes simplify the TS, meet regulatory 
    requirements for relocated TS, and implement the recommendations of 
    the Commission's Final Policy Statement on TS Improvements. Future 
    changes to these requirements will be controlled by 10 CFR 50.59. 
    The proposed changes are administrative in nature and do not involve 
    any modifications to any plant equipment or affect plant operation.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Do the changes create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes are administrative in nature, do not 
    involve any physical alterations to any plant equipment, and cause 
    no change in the method by which any safety-related system performs 
    its function.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        c. Do the changes involve a significant reduction in a margin of 
    safety?
        The proposed changes do not alter the basic regulatory requirements 
    and do not affect any safety analyses. Therefore, the proposed changes 
    do not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas & 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Theodore R. Quay
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-
    323,Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2,San Luis 
    Obispo County, California
    
        Date of amendment request: August 17, 1994 (Reference LAR 94-09)
        Description of amendment request: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant (DCPP) Unit Nos. 1 and 2 to change TS 3/4.4.9.1, ``Reactor 
    Coolant System - Pressure/Temperature Limits,'' Figures 3.4-2, 
    ``Reactor Coolant System Heatup Limitations - Applicable Up to 8 
    EFPY,'' and 3.4-3, ``Reactor Coolant System Cooldown Limitations - 
    Applicable Up to 8 EFPY,'' to extend the applicability up to 12 
    effective full-power years (EFPYs). TS 3/4.4.9.3, ``Overpressure 
    Protection Systems,'' would be revised to specify a new low-temperature 
    overprotection (LTOP) system actuation pressure setpoint. The 
    associated Bases would also be appropriately revised. Additionally, TS 
    3/4.1.2.2, ``Flow Paths - Operating,'' TS 3/4.1.2.4, ``Charging Pumps - 
    Operating,'' TS 3/4.4.1.3, ``Hot Shutdown,'' TS 3/4.4.1.4.1, ``Cold 
    Shutdown - Loops Filled,'' TS 3/4.4.9.3, and TS 3/4.5.3, ``Tavg Less 
    than 350 Degrees F,'' would be revised to specify a new LTOP system 
    enable temperature.
        (1) In TS 3/4.4.9.1, Figure 3.4-2, ``Reactor Coolant System Heatup 
    Limitations - Applicable Up to 8 EFPY,'' and Figure 3.4-3, ``Reactor 
    Coolant System Cooldown Limitations - Applicable Up to 8 EFPY,'' are 
    revised as follows:
        (a) The ``Controlling Materials'' for the pressure/temperature 
    curves are revised to reflect the current reactor vessel beltline 
    region limiting weld and plate materials. (b)The title for the figures 
    is changed to reflect the applicability of the pressure/temperature 
    curves for up to 12 EFPYs of service life.
        (2) The proposed changes to TS 3/4.4.9.3 are as follows:(a) The 
    LTOP enable temperature would be changed from 323 deg.F to 270 deg.F to 
    be consistent with Branch Technical Position (BTP) RSB 5-2, Revision 1, 
    Branch Position B.2.
        (b) LTOP system actuation pressure setpoint would be revised from 
    less than or equal to 450 psig to less than or equal to 435 psig.
        (3) TS 3/4.1.2.2, TS 3/4.1.2.4, TS 3/4.4.1.3, TS 3/4.4.1.4.1, TS 3/
    4.4.9.3, and TS 3/4.5.3 would be revised to change the LTOP enable 
    temperature from 323 deg.F to 270 deg.F to be consistent with BTP RSB 
    5-2, Revision 1, Branch Position B.2. TS Bases 3/4.4.9.1 would be 
    revised to delete a reference to Table 4.4-5, ``Reactor Vessel Material 
    Surveillance Program - Withdrawal Schedule.'' The table was deleted 
    from the TS in Amendments 54 and 53 issued in July 1990. Reference to 
    the table in Bases 3/4.4.9 was inadvertently not deleted. The 
    information in this table is currently contained in the Final Safety 
    Analysis Report (FSAR) Update.
        (4) TS Bases 3/4.4.9.3 would be revised to discuss limitations on 
    reactor coolant pump (RCP) and emergency core cooling system/chemical 
    and volume control system pump operation during low reactor coolant 
    system (RCS) temperature conditions.
        (5) The other affected TS Bases would also be revised.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes to Figures 3.4-2 and 3.4-3 of TS 3.4.9.1 
    and the associated Bases will extend the applicability of the RCS 
    heatup and cooldown pressure/temperature limits from 8 to 12 EFPY. 
    Since the level of reactor vessel embrittlement projected for 12 
    EFPY is bounded by that previously projected for 8 EFPY, the 
    proposed changes will not impact the probability of brittle fracture 
    of the vessel, and consequently not impact the consequences of an 
    accident.
        The present LTOP pressure setpoint was reviewed and found to be 
    acceptable and conservative for the extension of the pressure/
    temperature curves to 12 EFPY. However, as a result of issues 
    unrelated to the change in the applicability of the pressure/
    temperature curves, the LTOP actuation pressure setpoint is reduced. 
    The change accounts for pressure measurement error identified in NRC 
    IN [Information Notice] 93-58, a time delay in the LTOP system 
    actuation introduced as part of the installation of the Eagle 21 
    protection system, and additional conservatism incorporated into the 
    DCPP LTOP analysis. The changes to the pressure setpoint are 
    conservative and provide assurance that the maximum cold RCS 
    pressure will not be exceeded.
        The proposed change to TS 3/4.1.2.2, 3/4.1.2.4, 3/4.4.1.3, 3/
    4.4.9.3, and 3/4.5.3 will revise the LTOP enable temperature to be 
    consistent with the methodology and definition of ``low 
    temperature'' provided in BTP RSB 5-2 Revision 1. The proposed 
    changes do not involve physical alteration of the LTOP system or 
    change the method by which the LTOP system performs its function. 
    The proposed changes will benefit DCPP by expanding the RCS 
    pressure/temperature window, thereby increasing operator flexibility 
    during heatup and cooldown. This will decrease the probability of an 
    accident by decreasing the likelihood of an inadvertent PORV [power-
    operated relief valve] actuation.
        Deletion of reference to Table 4.4-5 from TS Bases 3/4.4.9 is 
    administrative in nature and does not affect plant operation.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes to TS 3.4.9.1 do not involve any physical 
    alteration to any plant system or change the method by which any 
    safety-related system performs its function. The probability of 
    catastrophic failure of the reactor vessel will not be changed as a 
    result of the extension of the curves to 12 EFPY.
        The present LTOP pressure setpoint was reviewed and found to be 
    acceptable and conservative for the extension of the pressure/
    temperature curves to 12 EFPY. However, as a result of issues 
    unrelated to the change in the applicability of the pressure/
    temperature curves, the LTOP actuation pressure setpoint is reduced. 
    The change accounts for pressure measurement error identified in IN 
    93-58, a time delay in the LTOP system actuation introduced as part 
    of the installation of the Eagle 21 protection system, and 
    additional conservatism incorporated into the DCPP LTOP analysis. 
    The changes to the pressure setpoint are conservative and provide 
    assurance that the maximum cold RCS pressure will not be exceeded.
        The proposed change to TS 3/4.1.2.2, 3/4.1.2.4, 3/4.4.1.3, 3/
    4.4.9.3, and 3/4.5.3 will revise the LTOP enable temperature to be 
    consistent with the methodology and definitions provided in BTP RSB 
    5-2, Revision 1. Additionally, the proposed changes will not affect 
    the ability of the LTOP system to provide pressure relief at low 
    temperatures, thereby maintaining the LTOP design basis.
        Deletion of reference to Table 4.4-5 from TS Bases 3/4.4.9 is 
    administrative in nature and does not result in physical alterations 
    or changes to the operation of the plant.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes to TS 3.4.9.1 will extend the applicability 
    of the RCS heatup and cooldown pressure/temperature limits to 12 
    EFPY, but will not physically change these limits. The pressure/
    temperature limits have been determined in accordance with 10 CFR 
    50, Appendix G, and include the safety margins with regard to 
    brittle fracture required by the ASME Code, Section III, Appendix G. 
    The RTndts determined for the reactor vessels at 12 EFPY are 
    lower than the values previously determined at 8 EFPY. Therefore, 
    there will be additional safety margin in the pressure/temperature 
    limits with respect to Appendix G requirements.
        The change in the LTOP pressure setpoint is conservative and 
    provides assurance that the current margin of safety is maintained. 
    The proposed change to TS 3/4.1.2.2, 3/4.1.2.4, 3/4.4.1.3, 3/
    4.4.9.3, and 3/4.5.3, will revise the LTOP enable temperature to be 
    consistent with the methodology and definitions provided in BTP RSB 
    5-2, Revision 1, which provides the requirements for reactor vessel 
    overpressurization protection at low temperatures.
        Deletion of reference to Table 4.4-5 from TS Bases 3/4.4.9 is an 
    administrative change and does not involve any physical alteration 
    to the plant.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas & 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Theodore R. Quay
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: August 12, 1994
        Description of amendment request: The amendment would revise the 
    Limiting Condition for Operation for the Emergency Core Cooling System 
    specified in Technical Specifications Section 3.5.1 and associated 
    Bases Section 3.4.5.1 to include a new ACTION statement in the event 
    that the High Pressure Coolant Injection system and one Core Spray 
    subsystem, and/or one Low Pressure Coolant Injection subsystem, are 
    inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS change does not involve any physical changes to 
    plant systems or components, nor does it affect the ability of the 
    Low pressure Coolant Injection (LPCI) Core Spray (CS), and High 
    Pressure Coolant Injection (HPCI) systems to respond to an accident. 
    These systems are not accident initiators, since their design 
    function is accident mitigation.
        This proposed TS change, which only addresses equipment status, 
    will not significantly increase the probability of occurrence of an 
    accident previously evaluated. The addition of the proposed ACTION 
    statement enables the plant not to implement TS Section 3.0.3, which 
    requires a plant shutdown, when the HPCI system is inoperable in 
    conjunction with one (1) CS subsystem, and/or one (1) LPCI 
    subsystem. The proposed TS change does not impact the operation of 
    any equipment important to safety. This proposed TS change does not 
    make physical modifications to the plant or to equipment, nor does 
    it impact any design requirements of the HPCI, CS, and LPCI systems. 
    The proposed TS change does not introduce any failure mechanisms of 
    a different type than those previously evaluated, since no physical 
    changes are being made to the facility. This proposed change will 
    not create any new failure modes which would cause plant equipment 
    to malfunction more frequently than previously evaluated.
        The basis for TS Sections 3.8.2.1 and 3.8.3.1, which specify 
    that four (4) independent divisions of Safeguard dc electrical power 
    shall be operable, or shall be restored to operability with 8 hours, 
    is to ensure that sufficient power is available to supply safety-
    related equipment required to safely shut down the plant, and to 
    provide for mitigation and control of accident conditions at the 
    plant. As discussed in Section 6.3.2 of the NRC Safety Evaluation 
    Report (SER), i.e., NUREG-0991, ``Safety Evaluation Report Related 
    to the Operation of Limerick Generating Station, Units 1 and 2,'' 
    dated August 1983, the most limiting single failure for the 
    Emergency Core Cooling System (ECCS), which includes all break 
    sizes, is the failure of the dc power system common to the HPCI 
    system, one (1) CS subsystem, and one (1) LPCI subsystem. Only one 
    (1) single failure is assumed to occur in the event of a Design 
    Basis Accident (DBA). Therefore, three (3) LPCI pumps, one (1) CS 
    subsystem, and the Automatic Depressurization (ADS) system would be 
    operable and available, for use in the event of a DBA, to provide 
    sufficient core cooling to safely shut down the plant. Although the 
    loss of Division 2 dc power specifically impacts the ``B'' LPCI and 
    ``B'' CS, the analysis performed in the NRC SER evaluates the number 
    of ECCS available for use in a DBA. Since the amount of available 
    core cooling is independent of which loop of LPCI or CS is assumed 
    to fail, this analysis is applicable to the loss of any division/
    loop of LPCI or CS. Therefore, the loss of the HPCI system, one (1) 
    CS subsystem, and/or one (1) LPCI subsystem is bounded by the 
    existing analysis. Since the loss of HPCI, one (1) CS subsystem, 
    and/or one (1) LPCI subsystem is an analyzed condition, and actions 
    associated with TS Section 3.0.3 are related to unanalyzed 
    conditions, the requirements of TS Section 3.0.3 are not applicable 
    to this scenario. Adding an ACTION statement, as proposed, identical 
    to the ACTION statement which currently applies to the loss of 
    Division 2 of Safeguard dc electrical power causes no change in the 
    consequences of any accidents previously evaluated. This proposed TS 
    change does not impact systems, structures, and components designed 
    to mitigate the consequences of an accident. In the event of an 
    accident, the plant configuration following the event will be within 
    the bounds of the existing analysis, and there will be no change in 
    the radiological consequences due to an accident.
        Therefore, the proposed TS change does not involve an increase 
    in the probability or consequences of an accident [previously] 
    evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS change does not require any physical changes to 
    plant systems or equipment, nor will it affect the ability of the 
    HPCI, CS, and LPCI systems from performing their design functions, 
    which is to mitigate the consequences of an accident. These systems 
    do not contribute to the initiation of an accident, since their 
    function is accident mitigation. This proposed TS change will not 
    introduce new equipment malfunction or failure modes. The proposed 
    TS change will not introduce any failure mechanisms of a different 
    type than those previously evaluated. The existing design basis for 
    the plant, as described in Section 6.3.2.5 of the LGS Updated Safety 
    Analysis Report (UFSAR) and Section 6.3.2 of the NRC SER, bounds the 
    condition proposed by this TS Change Request. Section 6.3.2 of the 
    NRC SER indicates that the most limiting single failure for the ECCS 
    is the loss of the dc system powering the HPCI, CS, and LPCI 
    systems. Assuming this failure, three (3) LPCI pumps, one (1) CS 
    subsystem, and the ADS would still be operable and available, for 
    use in the event of a DBA, to ensure adequate core cooling to safely 
    shut down the plant. Although the loss of Division 2 dc power 
    specifically affects ``B'' LPCI and ``B'' CS, the analysis performed 
    in the NRC SER evaluates the number of ECCS available for use in a 
    DBA. Since the amount of available core cooling is independent of 
    which loop of LPCI or CS is assumed to fail, this analysis is 
    applicable to the loss of any division/loop of LPCI or CS. Since the 
    loss of HPCI, one (1) CS subsystem, and/or one (1) LPCI subsystem, 
    is an analyzed condition, and the actions associated with TS Section 
    3.0.3 pertain to unanalyzed conditions, the requirements of TS 
    Section 3.0.3 do not apply to the condition proposed by this TS 
    Change Request.
        Therefore, the proposed TS change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        The proposed TS change [TS] does not involve any physical 
    changes to the design or functional requirements of the LPCI, CS, or 
    HPCI systems. These systems will continue to function as designed to 
    mitigate the consequences of an accident.
        This proposed TS change involves adding an additional ACTION 
    statement, and revising the associated supporting Bases section, to 
    specifically address the inoperability of the HPCI system in 
    conjunction with the inoperability of one (1) CS subsystem, and/or 
    one (1) LPCI subsystem. These systems would be inoperable in the 
    event of the loss of Division 2 of the Safeguard dc electrical power 
    supply. The Bases associated with Safeguard electrical power 
    systems, which provide power to equipment required to safely 
    shutdown the plant and to mitigate consequences of an accident, are 
    unchanged. The proposed TS change involves adding an ACTION 
    statement which is identical to the ACTION statement which addresses 
    the inoperability of Division 2 of Safeguard dc power, which is a 
    condition analyzed in the LGS UFSAR and NRC SER. Therefore, the 
    proposed TS change to include an additional ACTION statement does 
    not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Mohan C. Thadani, Acting
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: August 23, 1994
        Description of amendment request: This amendment would remove the 
    125/250 Vdc Class 1E Battery Load Cycle Table from Technical 
    Specifications, which is consistent with NUREG-1433, ``Standard 
    Technical Specifications.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed TS change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        This proposed change removes the repetitious 125/250 Vdc Class 
    1E Battery Load Cycle Table which is also found in the LGS Updated 
    Final Safety Analysis Report (UFSAR). The proposed change to TS does 
    not affect the requirement to perform surveillance testing and the 
    manner of performing surveillance testing is adequately described in 
    plant procedures. The UFSAR containing the Battery Load Cycle Table 
    and station procedures are maintained using the provisions of 10 CFR 
    50.59 and are subject to the change control process in the 
    Administrative Controls Section of the LGS TS Section 6.0. Since any 
    future changes to these controlled documents will be evaluated per 
    10 CFR 50.59, no [changes] (significant or insignificant) in the 
    probability or consequences of an accident previously evaluated will 
    be allowed. Therefore, this change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        This proposed change removes the repetitious 125/250 Vdc Class 
    1E Battery Load Cycle Table which is also found in the LGS Updated 
    Final Safety Analysis Report (UFSAR). This change will not alter the 
    plant configuration (no new or different type of equipment will be 
    installed) or make changes to methods governing normal plant 
    operations. This change will not impose different requirements and 
    adequate control of information will be maintained. The manner of 
    performing surveillance testing can be adequately described in plant 
    procedures. The proposed change will remove the table, and will not 
    alter assumptions made in the safety analysis and licensing basis. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        This proposed change removes the repetitious 125/250 Vdc Class 
    1E Battery Load Cycle Table which is also found in the LGS Updated 
    Final Safety Analysis Report (UFSAR). The change will not reduce the 
    margin of safety since the location of the Battery Table has no 
    impact on any safety analysis assumptions. Since all Battery Load 
    Table changes (i.e., UFSAR Changes) and procedure changes are 
    evaluated per the requirements of 10 CFR 50.59, no reduction 
    (significant or insignificant) in the margin of safety will be 
    allowed. Therefore, this change will not involve a significant 
    reduction in a margin of safety.
        The existing requirements for NRC review and approval of 
    revisions, in accordance with 10 CFR 50.90, to those details and 
    requirements proposed for deletion, do not have a specific margin of 
    safety upon which to evaluate. However, since the proposed change is 
    consistent with the BWR Standard Technical Specifications (NUREG-
    1433), revising the TS to reflect the approved level of detail and 
    requirements ensures no reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Mohan C. Thadani, Acting
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: August 5, 1994
        Description of amendment request: The proposed amendment 
    incorporates line item Technical Specification improvements listed in 
    Generic Letter 93-05 relevant to Emergency Diesel Generator (EDG) 
    surveillance requirements. The proposed amendment eliminates the 
    requirements to start EDGs with an inoperable offsite circuit(s) of AC 
    electrical power and adds a provision that eliminates required testing 
    of the remaining EDGs when one EDG is inoperable due to an inoperable 
    support system or an independently testable component with no potential 
    for common mode failure for the remaining EDGs. In addition, if testing 
    of the EDGs is required, then the surveillances will be performed 
    within 16 hours instead of 24 hours as currently specified.
        The proposed amendment also deletes the requirement to perform a 
    loss of offsite power (LOP) test following the 24-hour EDG endurance 
    run test. In its place, a hot restart test (no LOP load sequencing) 
    will be established.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        LCR 94-10
        The proposed changes in this License Change Request (LCR) have 
    been extensively reviewed by the NRC during the preparation of 
    NUREG-1366 and Generic Letter 93-05, and by [Public Service Electric 
    and Gas Company] PSE&G during the development and approval of this 
    LCR. The LCR revises the current ACTION statement of Technical 
    Specification 3.8.1.1 to eliminate testing of the unaffected 
    Emergency Diesel Generators (EDGs) upon loss of an offsite power 
    circuit(s) and/or an EDG. The basis for this testing was originally 
    to verify the reliability of the EDGs, however, as stated in NUREG-
    1366, industry experience has shown that excessive testing of the 
    EDGs has in fact reduced reliability.
        The EDG design and function remain as previously analyzed and 
    the EDG response during accident conditions is not affected. This 
    change will improve EDG performance by reducing the number of 
    unnecessary starts and by requiring more appropriate testing (within 
    16 hours instead of 24 hours) when there is a potential common mode 
    failure.
        These changes will not result in a significant increase in the 
    probability or consequences of a previously evaluated accident, nor 
    will it result in a significant reduction in a margin of safety.
        LCR 94-13
        The proposed changes in this License Change Request (LCR) have 
    been extensively reviewed by the NRC during the preparation of 
    NUREG-1366 and Generic Letter 93-05, and by PSE&G during the 
    development and approval of this LCR. Regulatory Guide 1.108, Rev. 
    1, states that the performance of a loss of Off-site Power (LOP) 
    test (Surveillance Requirement 4.8.1.1.2.h.4.b) immediately 
    following the 24 hour endurance run demonstrates that the Emergency 
    Diesel Generator (EDG) can start in the prescribed time when the EDG 
    is at its normal operating temperature. The purpose of performing 
    the LOP test immediately following the 24 hour endurance run is to 
    demonstrate the hot restart capability of the EDG at full load 
    conditions. However, demonstrating diesel generator hot restart 
    capability without loading the engine does not invalidate or reduce 
    the effectiveness of the hot restart test. Performance of this test 
    can be conducted in any plant condition since its performance at 
    power will have no adverse effect on plant operations.
        The LOP test will continue to be performed at standby conditions 
    to provide assurance that the EDG is capable of responding to a LOP 
    as assumed in the accident analyses.
        EDG design and function remain as previously analyzed. Their 
    response during accident conditions [is] not affected by these 
    changes. Therefore, no significant increase in the probability of an 
    accident previously evaluated results from these changes.
        2. Will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        LCR 94-10
        The elimination of the unnecessary EDG starts will not result in 
    any change in plant configuration or operation. Therefore, the 
    proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated or 
    analyzed.
        LCR 94-13
        The proposed revisions to the Technical Specifications do not 
    involve a physical change in any system configuration and do not 
    introduce new operating configurations. These changes will not 
    result in any net reduction in testing and will not affect EDG 
    reliability. This test may be performed in any plant condition since 
    its performance at power will have no adverse effect on plant 
    operations. Therefore, these changes do not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. Will not involve a significant reduction in a margin of 
    safety.
        LCR 94-10
        The changes proposed in this LCR do not reduce the ability of 
    any system or component to perform its safety related function. The 
    basis of NUREG-1366, Generic Letter 93-05 and the analysis performed 
    in support of this LCR is that the reduction in unnecessary EDG 
    starts can improve safety by diminishing challenges to plant systems 
    and reducing equipment wear or degradation. These proposed changes 
    involve only surveillance frequencies and do not change the method 
    of performing any surveillance. The operation of systems and 
    equipment remains unchanged. Therefore, eliminating unnecessary EDG 
    starts does not involve a reduction in the margin of safety.
        LCR 94-13
        Surveillance testing per the proposed Technical Specifications 
    would continue to demonstrate the ability of the EDGs to perform 
    their intended function of providing electrical power to the 
    emergency safety systems needed to mitigate design basis transients 
    consistent with the plant safety analyses. The margin of safety 
    demonstrated by the plant safety analyses is therefore not affected 
    by the proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: Mohan C. Thadani, Acting
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: August 19, 1994
        Description of amendment request: The proposed changes add a new 
    statement (b) to Limiting Condition for Operation (LCO) 3.1.3.2.1, Rod 
    Position Indication Systems, and reletters the existing action 
    statement (b) to (c). The new action (b) will read:
        With two or more analog rod position indicators per bank 
    inoperable, within one hour restore the inoperable rod position 
    indicator(s) to OPERABLE status or be in Hot Standby within the next 
    6 hours. A maximum of one rod position indicator per bank may remain 
    inoperable following the one hour, with Action (a) above being 
    applicable from the original entry time into the LCO.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The request (both proposed changes) does not change any 
    assumption or parameter assumed to function in any of the design/
    licensing basis analysis, and therefore the probability or 
    consequences of an accident previously evaluated are not increased. 
    The change, as described in section IB, [the addition of the new 
    action statement] incorporates into the applicable LCO the action 
    statement which is already taken under technical specification 
    3.0.3, and does not alter the operator response or response time.
        2. Does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed change does not introduce any design or physical 
    configuration changes to the facility which could create new 
    accident scenarios.
        3. Does not involve a significant reduction in a margin of 
    safety.
        As stated in response to question number 1 above, the change 
    does not change any assumption or parameter assumed to function in 
    any of the design/licensing basis analysis. No changes to the 
    operator response or operator response time is proposed, only that 
    the response is now taken under the confines of the LCO.
        Therefore, there is no reduction in any margin of safety from 
    the proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: Mohan C. Thadani, Acting
    
    South Carolina Electric & Gas Company, South Carolina Public 
    ServiceAuthority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: July 20, 1994, as supplemented September 
    20, 1994
        Description of amendment request: The proposed change would modify 
    the Virgil C. Summer Nuclear Station, Unit 1, (VCSNS) Technical 
    Specifications (TS) to allow alternative, equivalent testing of diesel 
    fuel used in the emergency diesel generators (EDG). These alternative 
    methods are necessary due to recent changes in Environmental Protection 
    Agency (EPA) Regulations that are designed to limit the use of high 
    sulfur fuels. The licensee also proposes to modify the VCSNS TS by 
    changing the revision level of WCAP-10216-P-A, ``Relaxation of Constant 
    Axial Offset Control - FQ Surveillance Technical Specification,'' 
    referenced in TS 6.9.1.11. This pertains to the FQ(z) TS (TS 3.2.1 and 
    3.2.2) and is necessary since Westinghouse revised their methodology in 
    determining FQ(z).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
        The change in testing methods for the EDG fuel oil has no impact 
    on the probability or consequences of any design basis accident. 
    These tests have been determined to be equivalent to the previously 
    approved testing methods and are needed due to changes in the EPA's 
    regulations regarding sulfur in motor vehicle fuels. The dye used to 
    identify high sulfur fuels will have no adverse affect on the 
    performance of the EDG's. The proposed testing assures a continued 
    high level of quality of the diesel fuel received and stored on 
    site.
        The change in revision level of a reference in TS section 
    6.9.1.11 has no impact on the probability of occurrence or 
    consequences of any design basis accident. All design and 
    performance criteria will continue to be met and no new single 
    failure mechanisms will be created. The change in revision level for 
    WCAP-10216-P-A does not involve any alterations to plant equipment 
    or procedures which could affect any operational modes or accident 
    precursors. This change only incorporates by reference, the 
    methodology for determining the penalty to be used in calculating 
    Core Operating Limits. This methodology allows the penalty to be 
    cycle specific and is primarily affected by the core configuration. 
    This penalty is used for normal operation and provides more 
    conservatism to the core operation for the cycle.
        2. [The proposed license amendment does not] create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The change in testing methods for the EDG fuel oil will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated. These tests have been determined 
    by the EPA and other organizations to be equivalent to the 
    previously approved testing methods. The effect of the blue dye, 
    used to identify high sulfur fuels, on the performance of the EDGs 
    has been evaluated and determined to be insignificant. The testing 
    proposed assures a continued high level of quality for the diesel 
    fuel received and stored on site.
        The change of revision level of a reference in TS section 
    6.9.1.11 has no impact on the probability of occurrence or 
    consequences of any design basis accident. All design and 
    performance criteria will continue to be met and no new single 
    failure mechanisms will be created. The change in revision level for 
    WCAP-10216-P-A does not involve any alterations to plant equipment 
    or procedures which could affect any operational modes or accident 
    precursors. This change only incorporates, by reference, the 
    methodology for determining the penalty to be used in calculating 
    Core Operating Limits. This methodology allows the penalty to be 
    cycle specific and is primarily affected by the core configuration. 
    This penalty is used for normal operation and provides more 
    conservatism to the core operation for the cycle.
        3. [The proposed license amendment does not] involve a 
    significant reduction in a margin of safety.
        The change in testing methods for the EDG fuel oil will not 
    involve a significant reduction in a margin of safety. The proposed 
    testing methods have been determined to be equivalent to the 
    previously approved testing methods. The test for sulfur assures 
    that the sulfur content is within the allowable range for weight-
    percent. The test for color and clarity assures that the fuel is 
    relatively free of water and particulate contaminants. The proposed 
    tests provide at least an equivalent level of quality and 
    repeatability for the fuel oil analysis, thus assuring that the 
    margin of safety is not reduced.
        The change in revision level of a reference in TS section 
    6.9.1.11 does not change the proposed reload design or safety 
    analysis limits for each cycle reload core. The associated change to 
    WCAP-10216-P-A due to the revision will be specifically evaluated 
    using approved reload design methods. The larger penalty actually 
    provides for an increase in margin during certain burnup ranges. 
    Since the safety analysis limits are unaffected, and the cycle 
    specific analysis will show that the analysis limits are met, the 
    change proposed will have no adverse impact on a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Fairfield County Library, 
    Garden and Washington Streets, Winnsboro, South Carolina 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: David B. Matthews
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: July 28, 1994
        Description of amendment requests: The licensee proposes revisions 
    to Technical Specification (TS) 3.9.8.1, ``Shutdown Cooling and Coolant 
    Circulation -- High Water Level,'' TS 3.9.8.2, ``Shutdown Cooling and 
    Coolant Circulation -- Low Water Level,'' and their Bases to facilitate 
    testing of low-pressure safety injection system components and permit 
    additional flexibility in scheduling maintenance on the shutdown 
    cooling system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No
        Limiting Conditions for Operation (LCO) in Technical 
    Specifications (TSs) 3.9.8.1 and 3.9.8.2 define the operability 
    requirements for the Shutdown Cooling (SDC) system during refueling 
    operations (Mode 6) while the water level above the top of the 
    reactor vessel flange is at least 23 feet and less than 23 feet, 
    respectively. The objective of these TSs is to ensure that (1) 
    sufficient cooling is available to remove decay heat, (2) the water 
    in the reactor vessel is maintained below 140 degrees Fahrenheit, 
    and (3) sufficient coolant circulation is maintained in the reactor 
    core to minimize boron stratification leading to a boron dilution 
    incident.
        The proposed TS changes affect the current limits imposed while 
    ensuring adherence to the basis of the TS. No plant modifications 
    are being made. The reactor cavity water level limitations and SDC 
    system required operating times are being changed based on plant 
    specific calculations and the objectives of the TSs are being 
    maintained.
        (1) reduce the water level where two trains of SDC are required 
    from 23 feet to 20 feet above the reactor pressure vessel flange,
        In the Bases Section 3/4.9.8, it is stated that ``With the 
    reactor vessel head removed and 23 feet of water above the reactor 
    pressure vessel flange, a large heat sink is available for core 
    cooling, thus in the event of a failure of the operating shutdown 
    cooling train, adequate time is provided to initiate emergency 
    procedures to cool the core.''
        In the Bases for the New Standard Technical Specifications, 
    ``NUREG 1432, Revision 0, dated September 30, 1992, Section B 3.9.4 
    it is stated that; ``The 23 ft level was selected because it 
    corresponds to the 23 ft requirement established for fuel movement 
    in LCO 3.9.6, ``Refueling Water Level.''
        Southern California Edison (Edison) calculations show that there 
    is a minimal difference in the time to boil due to the 3-foot change 
    in required water level. Therefore, adequate water is still 
    available to mitigate the consequences of losing SDC.
        (2) increase the time a required train of the SDC system may be 
    removed from service from up to 1 hour per 8-hour period to up to 2 
    hours per 8-hour period,
        (3) allow the SDC system to be removed from service to allow 
    testing of Low Pressure Safety Injection system components,
        The proposed TS changes the time the SDC train may be removed 
    from operation from up to 1 hour per 8-hour period to up to 2 hours 
    per 8-hour period, and allows removal of the SDC train from 
    operation for testing of the Low Pressure Safety Injection (LPSI) 
    system components as well as for core alterations in the vicinity of 
    the hot legs. The proposed TS change also imposes certain 
    restrictions to ensure operating the SDC system in accordance with 
    this proposed TS change is of no safety significance. These 
    restrictions are discussed separately below.
        When securing the only operating train of the SDC system, the 
    maximum Reactor Coolant System (RCS) temperature is maintained less 
    than or equal to 140 degrees Fahrenheit. The initial conditions and 
    heatup rate are selected such that the RCS temperature remains less 
    than or equal to 140 degrees Fahrenheit during the test. Therefore, 
    there is ample margin to boiling. Typical initial temperatures are 
    less than 100 degrees Fahrenheit.
        The water being injected by the LPSI system test is cool water 
    from the Refueling Water Storage Tank (RWST) and will increase the 
    available inventory providing the heat sink by several inches. The 
    two hours is sufficient time to align the system to test, perform 
    the test, and restore the train of SDC to operation prior to 
    exceeding 140 degrees Fahrenheit.
        No operations are permitted that would cause a reduction of the 
    RCS boron concentration. This minimizes the probability of an 
    inadvertent boron dilution event. The use of adequately borated 
    water for injection into the RCS during the test provides assurance 
    that the test itself cannot lead to a boron dilution event. When the 
    SDC system is operating, the minimum SDC flow rate of 2200 gpm 
    imposed by TS 4.9.8.1 and TS 4.9.8.2 is sufficient to ensure 
    complete mixing of the boron within the RCS.
        The LPSI component testing is only allowed when the reactor 
    cavity water level is maintained greater than or equal to 20 feet 
    above the reactor pressure vessel flange. This level ensures an 
    adequate heat sink to perform the LPSI pump suction header check 
    valve test.
        (4) allow for running 1 train of shutdown cooling with 
    additional requirements when the water level is less than 20 feet 
    but greater than 12 feet above the reactor pressure vessel flange,
        (5) add an action to be taken when operating 1 train of SDC with 
    less than 20 feet above the reactor pressure vessel flange when the 
    specified requirements are not met,
        In the event of a loss of SDC, the time to boil is reduced from 
    approximately 3.7 hours when the water level is 23 feet above the 
    reactor vessel flange to approximately 2.3 hours at 12 feet, 
    assuming the reactor has only been shutdown for 6 days. However, 
    this is ample time to close containment (less than 1 hour) and to 
    restore SDC or initiate alternative cooling (e.g., add water to the 
    cavity (approximately 1 hour)). Twelve feet of water above the 
    reactor vessel flange corresponds to 24 feet 8-7/8 inches above the 
    active fuel.
        Requiring the reactor to be shutdown for at least 6 days to have 
    only one train of SDC operable when the reactor cavity level is 
    between 20 feet and 12 feet above the reactor pressure vessel flange 
    ensures that the time to boil is greater than twice the time it 
    would take us to establish containment closure and to commence 
    reactor cavity fill with the required standby equipment.
        One train of SDC operating with a containment spray pump allows 
    for the high capacity LPSI pump to be the main standby pump capable 
    of filling the reactor cavity to at least 20 feet above the reactor 
    pressure vessel flange upon loss of SDC. The high pressure safety 
    injection pump will also be maintained ready to increase the water 
    level if needed. In support of this contingency the RWST will be 
    required to contain the volume of water required to raise the level 
    to 20 feet above the reactor vessel flange.... The reactor cavity 
    can be filled at a rate of approximately 4.0 inches per minute with 
    the LPSI pump.
        If operating one train of the SDC system with less than 20 feet 
    of water above the reactor pressure vessel flange and any of the 
    required conditions are not met, requiring immediate action to 
    establish greater than or equal to 20 feet of water above the 
    reactor pressure vessel flange ensures no time is wasted trying to 
    restore conditions that should be used to increase the volume of 
    water of the heat sink. By taking action to restore the level to 20 
    feet above the reactor pressure vessel flange the plant will be 
    placed in TS 3.9.8.1, which only requires one train of SDC to be 
    operable. Additionally, the core will not heat up while the water 
    level in the reactor cavity is being raised with cool water from the 
    RWST. This will provide additional time to either restore the one 
    train of SDC or take other actions to provide core cooling.
        A Probabilistic Risk Assessment (PRA), with (a) one train of the 
    SDC system operable with the reactor cavity water level greater than 
    or equal to 12 feet above the reactor pressure vessel flange, and 
    (b) one train of the SDC system operable with the reactor cavity 
    water level greater than or equal to 20 feet above the reactor 
    pressure vessel flange, showed that the operations in accordance 
    with the proposed TS would not significantly increase the 
    probabilities of inventory boiling and core damage.
        (6) delete the obsolete reference to the implementation of DCP 
    2-6863 and MMP 3-6863,
        This is an editorial change.
        (7) delete an obsolete footnote allowing removal of both trains 
    of SDC with the water less than 23 feet above the reactor vessel 
    flange from the Unit 3 TSs.
        This is an editorial change.
        Therefore, proposed changes 1 through 7 do not involve a 
    significant increase in the probability or consequences of an 
    accident.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different kind of 
    accident from any accident previously evaluated?
        Response: No
        (1) reduce the water level where two trains of SDC are required 
    from 23 feet to 20 feet above the reactor pressure vessel flange,
        (2) increase the time a required train of the SDC system may be 
    removed from service from up to 1 hour per 8-hour period to up to 2 
    hours per 8-hour period,
        (3) allow the SDC system to be removed from service to allow 
    testing of Low Pressure Safety Injection system components,
        (4) allow for running 1 train of shutdown cooling with 
    additional requirements when the water level is less than 20 feet 
    but greater than 12 feet above the reactor pressure vessel flange,
        (5) add an action to be taken when operating 1 train of SDC with 
    less than 20 feet above the reactor pressure vessel flange when the 
    specified requirements are not met,
        The Limiting Conditions for Operation (LCO) in Technical 
    Specifications (TSs) 3.9.8.1 and 3.9.8.2 define the operability 
    requirements for the SDC system during refueling operations (Mode 6) 
    while the water level above the top of the reactor vessel flange is 
    at least 23 feet and less than 23 feet, respectively. The objective 
    of the proposed TS changes is to ensure that the intent of the Bases 
    is maintained. [i.e., (1) sufficient cooling is available to remove 
    decay heat, (2) water in the reactor vessel is maintained below 140 
    degrees Fahrenheit, and (3) sufficient coolant circulation is 
    maintained in the reactor core to minimize boron stratification 
    leading to a boron dilution incident.]
        The proposed TS changes affect the current limits imposed while 
    ensuring adherence to the basis of the TS. No plant modifications 
    are being made. The reactor cavity water level limitations and SDC 
    system required operating times are being changed based on plant 
    specific calculations and the objective of the TSs are being 
    maintained. The added requirements and action statement facilitate 
    safe operation.
        (6) delete the obsolete reference to the implementation of DCP 
    2-6863 and MMP 3-6863, and
        This is an editorial change.
        (7) delete an obsolete footnote allowing removal of both trains 
    of SDC with the water less than 23 feet above the reactor vessel 
    flange from the Unit 3 TSs.
        This is an editorial change.
        Therefore, the operation of the facility in accordance with 
    proposed changes 1 through 7 does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No
        Limiting Conditions for Operation (LCO) in TSs 3.9.8.1 and 
    3.9.8.2 define the operability requirements for the SDC system 
    during refueling operations (Mode 6) while the water level above the 
    top of the reactor vessel flange is at least 23 feet and less than 
    23 feet, respectively. The objective of these TSs is to ensure that 
    (1) sufficient cooling is available to remove decay heat, (2) the 
    water in the reactor vessel is maintained below 140 degrees 
    Fahrenheit, and (3) sufficient coolant circulation is maintained in 
    the reactor core to minimize boron stratification leading to a boron 
    dilution incident.
        (1) reduce the water level where two trains of SDC are required 
    from 23 feet to 20 feet above the reactor pressure vessel flange,
        In the Bases Section 3/4.9.8, it is stated that ``With the 
    reactor vessel head removed and 23 feet of water above the reactor 
    pressure vessel flange, a large heat sink is available for core 
    cooling, thus in the event of a failure of the operating shutdown 
    cooling train, adequate time is provided to initiate emergency 
    procedures to cool the core.''
        In the Bases for the New Standard Technical Specifications, 
    ``NUREG 1432, Revision 0, dated September 30, 1992, Section B 3.9.4 
    it is stated that: ``The 23 ft level was selected because it 
    corresponds to the 23 ft requirement established for fuel movement 
    in LCO 3.9.6, ``Refueling Water Level.''
        Edison calculations show that there is a minimal difference in 
    the time to boil due to the 3-foot change in required water level. 
    Therefore, the margin of safety has not been significantly reduced.
        (2) increase the time a required train of the SDC system may be 
    removed from service from up to 1 hour per 8-hour period to up to 2 
    hours per 8-hour period,
        (3) allow the SDC system to be removed from service to allow 
    testing of Low Pressure Safety Injection system components,
        The proposed TS changes the time the SDC train may be removed 
    from operation from up to 1 hour per 8-hour period to up to 2 hours 
    per 8-hour period, and allows removal of the SDC train from 
    operation for testing of the LPSI system components as well as for 
    core alterations in the vicinity of the hot legs. The proposed TS 
    change also imposes certain restrictions to ensure operating the SDC 
    system in accordance with this proposed TS change is of no safety 
    significance. These restrictions are discussed separately below.
        When securing the only operating train of the SDC system, the 
    maximum RCS temperature is maintained less than or equal to 140 
    degrees Fahrenheit. The initial conditions and heatup rate are 
    selected such that RCS temperature remains less than or equal to 140 
    degrees Fahrenheit during the test. Therefore, there is ample margin 
    to boiling. Typical initial temperatures are less than 100 degrees 
    Fahrenheit.
        The water being injected by the LPSI system test is cool water 
    from the RWST and will increase the available inventory providing 
    the heat sink by several inches. The two hours is sufficient time to 
    align the system to test, perform the test, and restore the train of 
    SDC to operation prior to exceeding 140 degrees Fahrenheit.
        No operations are permitted that would cause a reduction of the 
    RCS boron concentration. This minimizes the probability of an 
    inadvertent boron dilution event. The use of adequately borated 
    water for injection into the RCS during the test provides assurance 
    that the test itself cannot lead to a boron dilution event. When the 
    SDC system is operating, the minimum SDC flow rate of 2200 gpm is 
    sufficient to ensure complete mixing of the boron within the RCS.
        The LPSI component testing is only allowed when the reactor 
    cavity water level is maintained greater than or equal to 20 feet 
    above the reactor pressure vessel flange. This level ensures an 
    adequate heat sink to perform the LPSI pump suction header check 
    valve test.
        The added requirements and the nature of the test provide 
    assurances that the water temperature will be maintained less than 
    140 degrees Fahrenheit and that boron stratification is prevented.
        (4) allow for running 1 train of shutdown cooling with 
    additional requirements when the water level is less than 20 feet 
    but greater than 12 feet above the reactor pressure vessel flange,
        (5) add an action to be taken when operating 1 train of SDC with 
    less than 20 feet above the reactor pressure vessel flange when the 
    specified requirements are not met,
        In the event of a loss of SDC, the time to boil is reduced from 
    approximately 3.7 hours at 23 feet to approximately 2.3 hours at 12 
    feet, when the reactor has only been shutdown for 6 days. However, 
    this is ample time to close containment (less than 1 hour), and to 
    restore SDC or initiate alternative cooling (e.g., add water to the 
    cavity (approximately 1 hour)).
        Requiring the reactor to be shutdown for at least 6 days to have 
    only one train of SDC operable when the reactor cavity level is 
    between 20 feet and 12 feet above the reactor pressure vessel flange 
    ensures that the time to boil is greater than twice the time it 
    would take us to establish containment closure and to commence 
    reactor cavity fill with the required standby equipment.
        One train of SDC operating with a containment spray pump allows 
    for the high capacity LPSI pump to be the main standby pump capable 
    of filling the reactor cavity to at least 20 feet above the reactor 
    pressure vessel flange upon loss of SDC. The high pressure safety 
    injection pump will also be maintained ready to increase the water 
    level if needed. In support of this contingency the RWST will be 
    required to contain the volume of water required to raise the level 
    to 20 feet above the reactor vessel flange. The reactor cavity can 
    be filled at a rate of approximately 4.0 inches per minute with the 
    LPSI pump.
        If operating one train of the SDC system with less than 20 feet 
    of water above the reactor pressure vessel flange and any of the 
    required conditions are not met, requiring immediate action to 
    establish greater than or equal to 20 feet of water above the 
    reactor pressure vessel flange ensures no time is wasted trying to 
    restore conditions that should be used to increase the volume of 
    water of the heat sink. By taking action to restore the level to 20 
    feet above the reactor pressure vessel flange the plant will be 
    placed in TS 3.9.8.1, which only requires one train of SDC to be 
    operable. Additionally, the core will not heat up while the reactor 
    cavity water level is being raised with cool water from the RWST. 
    This will provide additional time to either restore the one train of 
    SDC or take other actions to provide core cooling.
        A PRA showed that the operations in accordance with the proposed 
    TS did not significantly increase the probabilities of inventory 
    boiling and core damage.
        (6) delete the obsolete reference to the implementation of DCP 
    2-6863 and MMP 3-6863,
        This is an editorial change.
        (7) delete an obsolete footnote allowing removal of both trains 
    of SDC with the water less than 23 feet above the reactor vessel 
    flange from the Unit 3 TSs.
        This is an editorial change.
        Therefore, operation of the facility in accordance with proposed 
    changes 1 through 7 do not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
        Attorney for licensee: James A. Beoletto, Esquire, Southern 
    California Edison Company, P. O. Box 800, Rosemead, California 91770
        NRC Project Director: Theodore R. Quay
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: September 9, 1994 (TS 94-04)
        Description of amendment request: The proposed change would revise 
    specifications associated with the cold leg accumulators (CLAs). 
    Specifically, the proposed amendment would: (1) remove a footnote from 
    Specification 3.5.1.1.c that applied to Unit 2 Cycle 6 operation only; 
    (2) add a requirement to Specification 3.5.1.1 that power be removed 
    from the CLA isolation valve when the reactor coolant system pressure 
    is above 2000 psig; (3) modify Specification 3.5.1.1 Action Statement 
    a. to indicate that with a CLA inoperable for reasons other than the 
    boron concentration not being within limits, the CLA must be returned 
    to operable status within 1 hour or the plant placed in the hot standby 
    condition, and the pressurizer pressure reduced to 1000 psig or less 
    within the next 6 hours; (4) modify Specification 3.5.1.1 Action 
    Statement b. to indicate that with a CLA inoperable because the boron 
    concentration is not within limits, the boron concentration must be 
    restored to within limits within 72 hours or the plant placed in the 
    hot standby condition within the next 6 hours and the pressurizer 
    pressure reduced to 1000 psig or less within the next 6 hours; (5) 
    remove the wording from Specification 4.5.1.1.1.a.1 for using the 
    absence of alarms or level measurement as the technique used to verify 
    CLA volume and pressure; (6) add the requirement to Specification 
    4.5.1.1.1.a.2 to verify that the CLA isolation valve is ``fully open'' 
    rather than ``open;'' (7) modify Specification 4.5.1.1.1.b to show that 
    verification of boron concentration is not required for additions from 
    the refueling water storage tank, and add a footnote to indicate that 
    the verification is required only if the affected accumulator 
    experienced a volume increase; (8) modify Specification 4.5.1.1.1.c to 
    show that the test is satisfied by verifying that power is removed from 
    the isolation valve, not that the valve operator is disconnected by 
    removal of the breaker from the circuit; (9) delete Specification 
    4.5.1.1.1.d to verify that each CLA isolation valve opens automatically 
    when reactor coolant pressure exceeds the P-11 setpoint, and upon 
    receipt of a safety injection signal; (10) delete Specification 
    4.5.1.1.2 to verify the accumulator water level and pressure channels 
    operable by performing Channel Functional and Calibration tests, and 
    delete the related footnote; (11) change ``tanks'' to ``each cold leg 
    injection accumulator;'' and (12) revise the associated Bases where 
    necessary to reflect these changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes to TS 3.5.1.1 implement revised action 
    times for cold leg injection accumulator (CLA) inoperability. 
    Several other clarifications and enhancements have been incorporated 
    to provide consistency with the latest version of standard TSs 
    (NUREG-1431). The new action times provide a prompt one-hour action 
    to initiate unit shutdown for conditions that could prevent the 
    injection of a CLA into the core. For boron concentration outside 
    limits, a 72-hour action to restore CLA concentration is allowed 
    because the CLA can still perform the core injection safety 
    function. The removal of surveillance requirements (SRs) for 
    verifying automatic opening features for the CLA isolation valves 
    does not impact the required TS alignment that is assumed in the 
    safety analysis. The instrumentation calibration and functional test 
    SRs have also been removed based on the instrumentation only 
    providing CLA level and pressure indications for TS compliance and 
    not performing an accident mitigation function. The above changes do 
    not alter the required limits for CLA operability or system 
    configurations. These changes are consistent with NUREG-1431 and 
    provide acceptable flexability[sic] for CLA operability verification 
    and surveillance testing and reasonable actions for CLA 
    inoperability. Since no changes have been proposed that would change 
    the conditions assumed for the CLAs in the accident analysis, the 
    consequences of an accident will not be increased. The CLAs perform 
    accident mitigation functions and are not considered to be the 
    source of an accident. Therefore, since the plant configurations and 
    functions are unchanged by the proposed changes, the probability of 
    an accident will not be increased.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes clarify existing CLA operability 
    requirements, modify action times for CLA inoperability, enhance and 
    simplify SRs, and remove surveillances that are not required to 
    verify the CLA's ability to perform safety functions. None of these 
    changes affect the operation of the plant or the CLA configuration 
    and accident mitigation capabilities. Therefore, since the CLAs will 
    continue to support the plant as before, these proposed changes will 
    not create a new or different kind of accident.
        3. Involve a significant reduction in a margin of safety.
        The CLA requirements for volume, pressure, boron, and isolation 
    valve position are not changed by the proposed request. The CLAs 
    will continue to provide the same safety function capabilities as 
    assumed in the safety analysis. Therefore, no reduction in the 
    margin of safety will result from these chanes because CLA functions 
    are unchanged.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location:  Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: September 9, 1994 (TS 94-08)
        Description of amendment request: The proposed change would add 
    ``main steam vaults'' to the footnote of Surveillance Requirement 
    4.6.1.1. This would allow inspection of the valves, blind flanges, and 
    deactivated automatic valves located in the vaults that are required to 
    be in the closed position during accident conditions and that are 
    locked, sealed, or otherwise secured in the closed position, on a cold 
    shutdown frequency rather than every 31 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determine that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.93(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change will exempt containment isolation valves in 
    the east and west main steam valve vaults from examination every 
    thirty one days if those valves are locked, sealed or otherwise 
    secured. The valves and flanges that are located inside the main 
    steam valve vaults and are required to be closed during accident 
    conditions, will be verified in their required position during cold 
    shutdown and will be secured in this position. The environmental 
    conditions in these areas ensure they will be low traffic areas 
    where the probability of misalignment or manipulation is remote. 
    Loss of containment integrity is not considered to be an initiator 
    of any accident. This change does not affect any accident analysis 
    assumptions or results for SQN. Therefore, there is no increase in 
    the probability or consequences of an accident previously evaluated, 
    as a result of this change.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        This revision will not change any plant equipment, system 
    configurations, or accident assumptions. The appropriate components 
    in the valve vaults will continue to be verified in the closed 
    position and locked, sealed, or otherwise secured. The physical 
    congestion and high temperatures in the area will be effective in 
    maintaining this as a low traffic area that will contribute to the 
    low probability of misalignment or manipulation of these components 
    between inspections. Therefore, this change will not affect the 
    safety function of these components and will not create the 
    possibility of a new or different kind of accident.
        3. Involve a significant reduction in a margin of safety.
        The proposed change is consistent with current SQN accident 
    analysis assumptions since only the time interval between 
    performances of the surveillance is being extended. This change will 
    not impact any margin of safety.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: July 14, 1994
        Description of amendment request: The proposed changes to the 
    Technical Specifications would remove the remaining references to 
    cycle-specific parameters in Technical Specification 3.12.A.2 and 
    associated Technical Specification Figures 3.12-1A and 1B. These 
    figures and the control bank insertion limits are presently specified 
    in the Core Operating Limits Report (COLR). The NRC-approved 
    methodologies presently listed in the Technical Specifications are used 
    to calculate and evaluate the parameter limits presented in the COLR 
    for each reload core.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of Surry Power Station in accordance 
    with the Technical Specification changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The removal of the 
    remaining reference to cycle-specific core operating limits and 
    Technical Specification Figures 3.12-1A and 1B, from the Surry 
    Technical Specifications has no influence or impact on the 
    probability or consequences of any accident previously evaluated. 
    The proposed amendment is administrative in nature in that it 
    corrects omissions from a previously approved amendment. This change 
    has no impact on actions to be taken when or if limits are exceeded 
    as is required by the current Technical Specifications. Each 
    accident analysis addressed in the Surry UFSAR [Updated Final Safety 
    Analysis Report] will be examined with respect to changes in cycle-
    dependent parameters, which are determined by application of NRC-
    approved reload design methodologies. The impact of these parameter 
    changes on transient results is then evaluated to ensure that the 
    results remain bounded by respective transient analysis acceptance 
    criteria. This examination, which is performed per the requirements 
    of 10 CFR 50.59, ensures that future reloads will not involve an 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated. The removal of the remaining 
    reference to cycle-specific core operating limits and Technical 
    Specification Figures 3.12-1A and 1B has no influence or impact, nor 
    does it contribute in any way to the probability or consequences of 
    any accident previously evaluated. No safety-related equipment, 
    safety function, or plant operating characteristic will be altered 
    as a result of the proposed changes. This cycle-specific variable 
    (control bank insertion limits) is calculated using NRC approved 
    methods, and the results are submitted to the NRC for information in 
    accordance with Technical Specification 6.2. The Technical 
    Specifications will continue to require operation within the 
    required core operating limits, and appropriate actions will be 
    taken when or if any of these limits are exceeded. Therefore, the 
    proposed amendment does not in any way create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety. The 
    margin of safety is not affected by this administrative change which 
    removes the remaining reference to cycle-specific core operating 
    limits and Technical Specification Figures 3.12-1A and 1B from the 
    Technical Specifications. The margin of safety presently provided by 
    current Technical Specifications remains unchanged. Appropriate 
    measures exist to control the values of these cycle-specific limits. 
    The proposed amendment continues to require operation within the 
    core limits which were developed from the NRC-approved reload design 
    methodologies. Further, the actions to be taken when or if limits 
    are violated remain unchanged. Development of limits for future 
    reloads will continue to conform to those methods described in NRC-
    approved documentation. In addition, each reload requires a 10 CFR 
    50.59 safety review to assure that operation of the unit within the 
    cycle-specific limits will not involve a reduction in any margin of 
    safety. Therefore, the proposed changes are administrative in nature 
    and do not impact the operation of Surry in a manner that involves a 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Victor M. McCree (Acting)
    
    Virginia Electric and Power Company, Docket Nos. 50-280, 50-281, 
    50-338,50-339, Surry Power Station, Units No. 1 and No. 2 Surry 
    County,Virginia and North Anna Power Station, Units No. 1 and No. 
    2, LouisaCounty, Virginia
    
        Date of amendment request: September 6, 1994
        Description of amendment request: The proposed changes would revise 
    the Technical Specifications (TS) for Surry 1&2 and North Anna 1&2. 
    Specifically, the proposed changes would revise the: (1) Management 
    Safety Review Committee (MSRC) review responsibilities regarding safety 
    evaluations and Station Nuclear Safety and Operating Committee (SNSOC) 
    meeting minutes and reports, and (2) SNSOC review responsibilities for 
    procedure changes. However, the changes now also state that the MSRC 
    will review safety evaluations, and the SNSOC will review procedure 
    changes, as programmatically discussed in the Updated Final Safety 
    Analysis Report (UFSAR).
        The licensee's proposed changes revise and supersede the licensee's 
    original proposed changes dated December 27, 1993 and noticed in the 
    Federal Register on February 16, 1994, (59 FR 7700) for NA-1&2, and 
    March 16, 1994 (59 FR 12371) for Surry 1 & 2.
        The North Anna and Surry Power Station Technical Specifications 
    presently address the organization and responsibilities of both the 
    onsite and offsite review groups, the SNSOC and the MSRC, respectively. 
    The responsibilities of the SNSOC include the review of new procedures 
    and changes to procedures that affect nuclear safety. The MSRC review 
    responsibilities include the review of safety evaluations and SNSOC 
    meeting minutes and reports. It is proposed that the extent of these 
    review activities be revised in the Technical Specifications to ensure 
    the two review groups are focusing on nuclear safety issues and not 
    spending an unnecessary amount of time on administrative activities of 
    minimal safety significance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        [Specifically, operation in accordance with the proposed 
    Technical Specifications changes] will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. As administrative 
    changes, the proposed Technical Specifications changes have no 
    direct or indirect effect on accident precursors. No plant 
    modifications are being implemented and operation of the plant is 
    unchanged. SNSOC review of new procedures and procedure changes that 
    require a safety evaluation ensures that activities that could 
    affect nuclear safety are being properly reviewed. The MSRC's 
    overview of representative samples of safety evaluations and SNSOC 
    meeting minutes and reports based on performance ensures these 
    programs are being properly implemented and nuclear safety is not 
    being compromised; or
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated since physical modifications 
    are not involved and systems and components will be operated as 
    before the change. The proposed changes are wholly administrative in 
    nature and have no impact on plant operations or accident 
    considerations. These changes modify the scope of SNSOC review of 
    procedure changes and MSRC's review functions concerning safety 
    evaluations and SNSOC meeting minutes and reports. Procedure changes 
    will continue to receive management review in accordance with 
    administrative procedures, however, only changes that require a 
    safety evaluation will require SNSOC approval. MSRC review of 
    representatives samples of safety evaluations and SNSOC meeting 
    minutes and reports based on performance will continue to provide 
    adequate assurance that nuclear safety is being properly considered; 
    or
        3. Involve a significant reduction in a margin of safety as 
    defined in the basis of any Technical Specification since the 
    responsibilities of the SNSOC and MSRC are not addressed by the 
    existing Technical Specification Bases, nor are review requirements 
    for procedures. The proposed changes are administrative in nature 
    and have no impact on, nor were they considered in, existing UFSAR 
    accident analyses. Safety significant procedure changes, i.e., 
    changes that require a safety evaluation to be prepared, will 
    continue to be reviewed by SNSOC, as will new procedures. Procedure 
    changes still require cognizant management approval and preparation 
    of an activity screening to determine whether or not the change 
    impacts nuclear safety. This ensures activities important to nuclear 
    safety are being appropriately reviewed. The effectiveness of the 
    safety evaluation program, and the thoroughness of SNSOC meetings 
    and reports will be assured through the MSRC's plant overview 
    function which is based on observed performance.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185, and The Alderman 
    Library, Special Collections Department, University of Virginia, 
    Charlottesville, Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Victor McCree, Acting
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: August 24, 1994
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    3.1.b.1 and Figure TS 3.1-4 regarding Low Temperature Overpressure 
    (LTOP) protection for the reactor coolant pressure boundary. Currently, 
    the TS specify the LTOP requirements through the end of operating cycle 
    20 or 17.14 effective full power years. The proposed change extends the 
    LTOP requirements through the end of operating cycle 21 or 18.40 
    effective full power years. The Basis Section would also be modified to 
    reflect these changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        The proposed change was reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed change will not:
        1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The use of RG 1.99, Revision 2, Regulatory Position C.2 does not 
    modify the reactor coolant system pressure boundary, nor make any 
    physical changes to the facility design, material, construction 
    standards, or setpoints. The probability of a LTOP event occurring 
    is independent of the pressure temperature limits for the RCS 
    pressure boundary. Therefore, the probability of a LTOP event 
    occurring remains unchanged.
        The use of predicted fluence values through the end of operating 
    cycle 21 is appropriately considered within the calculations in 
    accordance with standard industry methodology previously docketed 
    under WCAP 13227. Revised flux values were used for Cycles 16, 17, 
    18 and 19 based on actual core reload designs. Previous cycles flux 
    values are the same as reported in WCAP 12333.
        The calculation of pressure temperature limits in accordance 
    with approved regulatory methods provides assurance that reactor 
    pressure vessel fracture toughness requirements are met and the 
    integrity of the RCS pressure boundary is maintained. Similar 
    methodology was used in calculations to support approved amendment 
    108 to the Kewaunee Technical Specifications dated April 7, 1994.
        The use of Regulatory Position C.2 and fluence values through 
    EOC 21 meet previously established criteria for protection of the 
    health and safety of the public. The consequences of a LTOP 
    transient therefore, remain unchanged.
        2) create the possibility of a new or different type of accident 
    from an accident previously evaluated.
        The use of Regulatory Position C.2 and fluence through EOC 21 
    does not modify the reactor coolant system pressure boundary, nor 
    make any physical changes to the LTOP setpoint or system design.
        Therefore, no new failure mechanisms are created that could 
    create the possibility of an accident of a new or different type.
        3) involve a significant reduction in the margin of safety.
        The Appendix G pressure temperature limitations are calculated 
    in accordance with regulatory requirements and calculational 
    limitations specified in RG 1.99, Revision 2. RG 1.99, Revision 2, 
    is an acceptable method for implementing the requirements of 10 CFR 
    50 Appendices G and H. Similar methodology was used in calculations 
    to support approved amendment 108 dated April 7, 1994. The reactor 
    coolant pump starting restrictions of TS 3.1.a.1.c remain in place.
        The revised calculations meet the NRC acceptance criteria for 
    the LTOP setpoint and system design as described in NRC Safety 
    Evaluation Report (SER) dated September 6, 1985 which concluded that 
    ``the spectrum of postulated pressure transients would be 
    mitigated...such that the temperature pressure limits of Appendix G 
    to 10 CFR 50 are maintained.''
        The use of Regulatory Position C.2, meets previously established 
    criteria for the pressure temperature limits for the LTOP system and 
    setpoint. Thus, the margin of safety as described in the NRC SER is 
    not reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: John N. Hannon
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: September 7, 1994
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specifications 
    (TS) by adding two new sections, TS Section 3.0 and TS Section 4.0, 
    with associated bases. TS Section 3.0 would establish the general 
    requirements applicable to each of the Limiting Conditions for 
    Operation (LCOs) within Section 3 of the KNPP TS. TS Section 4.0 would 
    establish the general requirements applicable to Surveillance 
    Requirements. The new requirements of TS 4.0.b would also affect TS 
    Sections 4.5, 4.6, 4.7, and Tables TS 4.1-2 and 4.1-3. The proposed TS 
    amendment incorporates guidance statements similar to Section 3.0/4.0 
    of NUREG-0452, ``Standard Technical Specifications for Westinghouse 
    Pressurized Water Reactors.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        The proposed changes were reviewed in accordance with the 
    provision of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The likelihood that an accident will occur is neither increased 
    or decreased by these TS changes. These TS changes will not impact 
    the function or method of operation of plant equipment. Thus, there 
    is not a significant increase in the probability of a previously 
    analyzed accident due to these changes. No systems, equipment, or 
    components are affected by the proposed changes. Thus, the 
    consequences of the malfunction of equipment important to safety 
    previously evaluated in the Updated Safety Analysis Report (USAR) 
    are not increased by these changes.
        The proposed changes have no impact on accident initiators or 
    plant equipment, and thus, do not affect the probabilities or 
    consequences of an accident.
        These changes are consistent with the requirements established 
    in the Westinghouse STS. Therefore, the proposed changes will not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed TS changes would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The proposed changes do not involve changes to the 
    physical plant or operations. Since these changes do not contribute 
    to accident initiation, they do not produce a new accident scenario 
    or produce a new type of equipment malfunction. Also, these changes 
    do not alter any existing accident scenarios; they do not affect 
    equipment or its operation, and thus, do not create the possibility 
    of a new or different kind of accident.
        3) involve a significant reduction in the margin of safety.
        Operation of the facility in accordance with the proposed TS 
    would not involve a significant reduction in a margin of safety. The 
    proposed changes do not affect plant equipment or operation. Safety 
    limits and limiting safety system settings are not affected by these 
    proposed changes. These changes are consistent with the Westinghouse 
    STS.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: John N. Hannon
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County,North Carolina
    
        Date of amendments request: September 9, 1994 Brief description of 
    amendments request: The amendments change the Technical Specifications 
    to revise the frequency for verifying the position of the drywell-
    suppression chamber vacuum breakers when the position indication is not 
    operable from at least once every 72 hours to at least once every 14 
    days.Date of publication of individual notice in Federal Register: 
    September 16, 1994 (59 FR 47648)
        Expiration date of individual notice: October 3, 1994
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: September 8, 1994
        Brief description of amendment: The proposed amendment would modify 
    Technical Specification 3.10.2, to permit the bypassing of the rod 
    withdrawal limiter notch constraints while performing fuel power 
    suppression testing. This modification to the technical specification 
    will allow River Bend Station to search for and identify the location 
    of leaking fuel bundles, during power operating conditions, so that 
    appropriate actions can be taken to prevent further degradation.
        Date of publication of individual notice in Federal Register: 
    September 16, 1994 (59 FR 47652)
        Expiration date of individual notice: October 17, 1994
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: September 12, 1994
        Brief description of amendment: The proposed amendment would revise 
    the formula for calculating the average power range monitor (APRM) flow 
    biased simulated thermal power-high reactor trip and flow biased 
    neutron flux-upscale control rod block trip setpoints T-factor 
    specified in Technical Specification (TS) 3/4.2.2. The proposed changes 
    are necessary to support implementation of recommendations contained in 
    NRC Generic Letter 94-02, ``Long-Term Solutions and Upgrade of Interim 
    Operating Recommendations for Thermal-Hydraulic Instabilities in 
    Boiling Water Reactors.''
        Date of publication of individual notice in Federal Register: 
    September 21, 1994 (59 FR 48456)
        Expiration date of individual notice:  October 21, 1994
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: September 9, 1994
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to modify surveillance requirements 
    by increasing the acceptance criterion for the closure of the main 
    steam isolation valves from 5 seconds to 10 seconds.
        Date of publication of individual notice in Federal Register: 
    September 19, 1994 (59 FR 47960).
        Expiration date of individual notice: October 19, 1994
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: September 8, 1994 (TS 94-14)
        Brief description of amendments: The amendment would separate the 
    portion of the steam generator tubing from the end of the tube up to 
    the start of the tube-to-tubesheet weld from the remainder of the tube 
    for the purposes of sample selection and repair when defects are found 
    in this section of a steam generator tube.
        Date of publication of individual notice in the Federal 
    Register:September 19, 1994 (59 FR 47962)
        Expiration date of individual notice: October 19, 1994
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennesee 37402.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529 and STN 50-530, Palo Verde Nuclear Generating Station, Unit 
    Nos. 1, 2 and 3, Maricopa County, Arizona
    
        Date of application for amendments: August 5, 1993
        Brief description of amendments: The amendments change the phrase 
    ``Pressurizer Pressure - Wide Range'' to ``Reactor Coolant System 
    Pressure - Wide Range'' in item 4 of TS Table 3.3-10 and item 4 of 
    Table 4.3-7. These amendments will clarify the instrumentation required 
    and eliminate potential confusion between the reactor coolant system 
    pressure instruments and the pressurizer pressure instruments.
        Date of issuance: September 21, 1994
        Effective date: September 21, 1994
        Amendment Nos.: 81, 68, and 53
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 29, 1993 (58 
    FR 50962) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 21, 1994. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: June 8, 1994
        Brief description of amendments: The amendments revise Technical 
    Specification Section 4.7.1.2.c to extend the interval for three 
    Auxiliary Feedwater surveillance requirements from 18 to 24 months.
        Date of issuance: September 26, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 197 and 174
        Facility Operating License No. DPR-53 and DPR-69: Amendment revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42334) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated September 26, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location:  Calvert County Library, 
    Prince Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: November 2, 1993, as 
    supplemented on June 22, 1994
        Brief description of amendments: The amendments revise the 
    Technical Specifications regarding surveillance requirements associated 
    with the emergency diesel generators (EDGs) which include the 
    following: 1) the surveillance interval is extended from 18 months to 
    24 months which is the current refueling cycle; 2) removes the 
    requirement to verify the EDGs speed; 3) exempts sequencer testing in 
    Modes 5 and 6; 4) deletes the reference to the specific 2000 hour 
    rating of the EDGs; and 5) allows the EDGs to be prelubricated prior to 
    being started in accordance with the vendors recommendation.
        Date of issuance: September 27, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 198 and 175
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64599) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated September 27, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: April 29, 1994
        Brief description of amendment: The amendment revises surveillance 
    intervals associated with initiation of auxiliary feedwater on steam 
    generator water level (low-low) and on trip of the main feedwater 
    pumps. These revisions are being made in accordance with the guidance 
    provided by Generic Letter 91-04, ``Changes in Technical Specification 
    Surveillance Intervals to Accommodate a 24-Month Fuel Cycle.''
        Date of issuance:  September 23, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 175
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42335) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 23, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment:  December 10, 1993, as 
    supplemented by letter dated August 11, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) Section 5.3.A., ``Reactor Core,'' to allow the use 
    of VANTAGE + fuel with ZIRLO cladding and of fuel with filler rods to 
    permit fuel reconstitution. The amendment also revises the Basis for TS 
    Section 2.1, ``Safety Limit: Reactor Core,'' to more accurately 
    describe the basis of the departure from nucleate boiling correlations 
    and how they are applied to ensure that the design criteria are met.
        Date of issuance:  September 29, 1994
        Effective date:  As of the date of issuance to be implemented 
    within 30 days.
        Amendment No.: 176
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10003) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 29, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Dairyland Power Cooperative, Docket No. 50-409, La Crosse Boiling 
    Water Reactor, La Crosse, Wisconsin
    
        Date of application for amendment: November 5, 1993 (Reference LAC-
    13320) as supplemented August 3, 1994, (Reference LAC-13420).
        Brief description of amendment: This amendment modified the 
    Technical Specifications (TS) incorporated in Possession-Only License 
    No. DPR-45 in accordance with a revision of 10 CFR Part 20 (56 FR 
    23360). In addition, there were minor clerical changes to correct 
    oversights from previous amendments.
        Date of issuance: September 27, 1994.
        Effective date: This license amendment is effective as of the date 
    of its issuance and must be fully implemented no later than 30 days 
    from the date of issuance.
        Amendment No.: 68.Possession-Only License No. DPR-9: The amendment 
    revised the TS.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    618) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 27, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: La Crosse Public Library, 800 
    Main Street, La Crosse, Wisconsin 54601.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments:  November 11, 1993, as 
    supplemented February 23, April 12 and July 29, 1994.
        Brief description of amendments: The amendments reflect the 
    consolidation of the Quality Verification Department with the Nuclear 
    Generation Department that realigned the Nuclear Safety Review Board to 
    report to the Senior Nuclear Officer, change a reference from Semi-
    Annual to Annual, change an organizational unit term from ``group'' to 
    ``division,'' modify titles of positions designated to approve 
    modifications and clarify the responsibilities of the Safety Assurance 
    Manager.
        Date of issuance: September 23, 1994
        Effective date: September 23, 1994
        Amendment Nos.: 124 and 118
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    618) The February 23, April 12 and July 29, 1994 letters provided 
    clarifying information that did not change the scope of the November 
    11, 1993, application and the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated September 23, 
    1994.No significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: November 11, 1993, and 
    supplemented February 23, April 12 and July 29, 1994.
        Brief description of amendments: The amendments reflect the 
    consolidation of the Quality Verification Department with the Nuclear 
    Generation Department that realigned the Nuclear Safety Review Board to 
    report to the Senior Nuclear Officer, change a reference from Semi-
    Annual to Annual, change an organizational unit term from ``group'' to 
    ``division,'' modify titles of positions designated to approve 
    modifications and clarify the responsibilities of the Safety Assurance 
    Manager.
        Date of issuance: September 22, 1994
        Effective date: September 22, 1994
        Amendment Nos.: 148 and 130
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 19, 1994 (59 FR 
    2865) The February 23, April 12 and July 29, 1994, letters provided 
    clarifying information that did not change the scope of the November 
    11, 1993, application and the initial proposed no significant hazards 
    considerationdetermination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated September 22, 
    1994. No significant hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments:  June 2, 1994
        Brief description of amendments: These amendments revise the 
    Appendix A TSs relating to reactor coolant leakage and leakage 
    detection systems in an effort to bring TS sections 3/4.4.6.1 and 3/
    4.4.6.2 closer to NRC's Improved Standard TSs. A new TS, Section 3/
    4.5.5 for Unit 1 and 3/4.5.4 for Unit 2, is added to address Seal 
    Injection Flow.
        Date of issuance:  September 22, 1994
        Effective date: September 22, 1994
        Amendment Nos.: 183 and 64
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39585) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 22, 1994No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: February 9, 1993, as supplemented by 
    letter dated July 22, 1994.
        Brief description of amendment: The amendment changed the Appendix 
    A Technical Specifications by revising Specifications 3.0.4, 4.0.3, and 
    4.0.4 in accordance with the intent of Generic Letter 87-09.
        Date of issuance:  September 20, 1994
        Effective date: September 20, 1994
        Amendment No.: 99
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42341) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 20, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: April 28, 1994, and 
    supplemented by letter dated July 29, 1994.
        Brief description of amendments: The proposed amendments would 
    revise Technical Specification (TS) 3/4.8.1.1, ``AC Sources 
    Operating,'' and the associated TS Bases for demonstrating the 
    operability of the diesel generators (DGs), based upon the following 
    NRC guidelines:A. Generic Letter (GL) 93-05, ``Line-Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operation.'' B. Regulatory Guide (RG) 1.9, 
    Revision 3, ``Selection, Design, Qualification, and Testing of 
    Emergency Diesel Generator Units Used as Class 1E Onsite Electric Power 
    Systems at Nuclear Power Plants,''
        Date of issuance: September 21, 1994
        Effective date: September 21, 1994
        Amendment Nos.: 75 and 54
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated September 21, 1994.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments:  June 24, 1994.
        Brief description of amendments: The amendments revise the values 
    of Z and S in Technical Specification 2.2-1 for the Pressurizer 
    Pressure-Low and -High trip set-points (Table 2.2-1, Functional Units 9 
    and 10) to allow the use of Tobar, Veritrak, or Rosemount pressure 
    transmitters.
        Date of issuance: September 22, 1994
        Effective date: September 22, 1994
        Amendment Nos.: 76 and 55
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 22, 1994 (59 FR 
    43143) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 22, 1994. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket No. 
    50-321, Edwin I. Hatch Nuclear Plant, Unit 1, Appling County, 
    Georgia
    
        Date of application for amendment: August 16, 1994, as supplemented 
    September 20, 1994
        Brief description of amendments: The amendment makes a one-time 
    change to Technical Specification (TS) 3.9.C for Hatch Unit 1 regarding 
    the emergency diesel generator (DG) operability requirements during 
    reactor shutdown conditions. Current TS 3.9.C requires that two DGs be 
    operable during reactor shutdown when a core or containment cooling 
    system is required to be operable. The amendment revises the current 
    requirement such that only one emergency DG is required to be aligned 
    to its associated core or containment cooling system during a specific 
    time of the outage. During this time period the decay heat removal 
    (DHR) system will be in service. The DHR system, which is completely 
    independent of the existing shutdown cooling system, is powered by the 
    Baxley substation and has its own DG as a backup power supply.
        Date of issuance: September 26, 1994
        Effective date: September 26, 1994
        Amendment Nos.: 194
        Facility Operating License Nos. DPR-57 and NPF-5. Amendment revised 
    the Technical Specifications. The September 20, 1994, letter provided 
    additional information that did not change the scope of the August 16, 
    1994, application and the initial proposed no significant hazards 
    consideration determination.
        Date of initial notice in Federal Register: August 26, 1994The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated September 26, 1994.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: April 19, 1994
        Brief description of amendment: The amendment updates and clarifies 
    Technical Specification (TS) 3.4.B.1 to be consistent with TSs 1.39 and 
    4.3.D. It addresses electromatic relief valve operability/bypassing 
    during system pressure testing, including system leakage and 
    hydrostatic test, with the reactor vessel solid, core not critical, and 
    core reactivity limits satisfied.
        Date of issuance: September 27, 1994
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 170
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27056) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated September 27, 1994. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, New Jersey 
    08753.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: February 22, 1994
        Brief description of amendments: The amendments revise the 
    Technical Specifications to reduce surveillance requirements for 
    testing during power operation in the areas of control rod movement 
    testing, radiation monitors, containment spray system, hydrogen 
    recombiners, emergency diesel generators, special test exceptions - 
    shutdown margin, and radioactive effluents - waste gas storage tanks.
        Date of issuance: September 28, 1994
        Effective date: September 28, 1994
        Amendment Nos.: 183 & 168
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14890) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 28, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 18, 1994
        Brief description of amendment: The amendment revises the current 
    surveillance frequency that verifies area temperature limits. The 
    revised surveillance requirement will verify area temperature limits at 
    least once per 7 days when the temperature monitor (datalogger) alarm 
    is operable, and at least once per 12 hours when the datalogger alarm 
    is inoperable.
        Date of issuance: September 22, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 95
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39593) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 22, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Community-Technical College, Thames Valley Campus, 574 New London 
    Turnpike, Norwich, Connecticut 06360.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments:  August 29, 1994 (Reference LAR 
    94-10)
        Brief description of amendments: The proposed amendments revise the 
    combined Technical Specifications (TS) for the Diablo Canyon Power 
    Plant Unit Nos. 1 and 2 to specify an alternate method of determining 
    water and sediment content for new diesel fuel oil as specified in TS 
    3/4.8.1.1, ``A.C. Sources - Operating.'' Specifically, TS 
    4.8.1.1.3c.1(d) is revised to allow new fuel oil to be tested using a 
    ``clear and bright'' test or a quantitative test that verifies a water 
    and sediment content less than or equal to 0.05 volume percent when the 
    oil is tested in accordance with ASTM D1796-83.
        Date of issuance: September 23, 1994
        Effective date: September 23, 1994
        Amendment Nos.: 95 and 94
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.Public comments requested as to 
    proposed no significant hazards consideration: Yes (59 FR 46453, dated 
    September 8, 1994). The notice provided an opportunity to submit 
    comments on the Commission's proposed no significant hazard 
    consideration determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by October 7, 
    1994, but stated that, if the Commission makes a final no significant 
    hazards consideration determination, any such hearing would take place 
    after issuance of the amendments.
        The Commission's related evaluation of the amendments, finding of 
    exigent circumstances, and final determination of no significant 
    hazards consideration is contained in a Safety Evaluation dated 
    September 23, 1994.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P. O. Box 7442, San Francisco, California 94120
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments:  October 29, 1992
        Brief description of amendments: These amendments revise the 
    Technical Specification by adding an alternate method of ensuring that 
    power to the safety injection tank vent valves is removed. The existing 
    method verifies that the fuses are removed. The alternate method 
    verifies that the disconnect switches are in the open position.
        Date of issuance: September 27, 1994
        Effective date: As of the date of its issuance.
        Amendment Nos.: 112 and 101
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 17, 1993 (58 
    FR 8783) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 27, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: April 4, 1994 (TS 322)
        Brief description of amendment: The amendments eliminate the 
    requirements in the Technical Specifications (TS) for automatic 
    actuation of the following functions upon Main Steamline Radiation 
    Monitor (MSRM) detection of a high radiation condition in the main 
    steamlines:(1) reactor scram (2) main steam isolation valve closure(3) 
    main steam line drain valve closure(4) reactor recirculation sample 
    line valve closure(5) main condenser mechanical vacuum pump isolation 
    and trip
        Date of issuance: September 27, 1994
        Effective date: September 27, 1994
        Amendment Nos.: 212, 227 and 185
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29636) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 27, 1994.No 
    significant hazards consideration comments received: None
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: March 19, 1992
        Brief description of amendment: This amendment revised Technical 
    Specifications to incorporate clarifications and corrections. These 
    changes were administrative and not safety significant.
        Date of issuance: September 21, 1994
        Effective date: date of issuance, to be implemented within 90 days
        Amendment No. 66
        Facility Operating License No. NPF-58. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 8, 1992 (57 FR 
    30260) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 21, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: May 26, 1994 as supplemented 
    July 11, 1994, and August 1, 1994.
        Brief description of amendments: Point Beach Nuclear Plant is 
    installing two additional emergency diesel generators and reconfiguring 
    portions of the 4160-Volt emergency electrical power system. The 
    amendment revised the Point Beach Nuclear Plant Technical 
    Specifications (TS) to establish the requirements for the electrical 
    systems at Point Beach such that the TS will provide the appropriate 
    guidance for all interim configurations and the final configuration. 
    The majority of changes were incorporated in TS Section 15.3.7, 
    ``Auxiliary Electrical Systems.'' Other Sections modified were 15.3.0, 
    ``General Considerations,'' 15.3.14, ``Fire Protection System,'' and 
    15.4.6, ``Emergency Power System Periodic Tests.''
        Date of issuance:  September 23, 1994
        Effective date: immediately, to be implemented within 45 days
        Amendment Nos.: 152 and 156
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37092) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 23, 1994.The July 11, 
    1994, and August 1, 1994, submittals provided additional supplemental 
    information that did not change the initial proposed no significant 
    hazards consideration determination.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: August 9, 1994, as supplemented 
    on August 19, 1994.
        Brief description of amendments: These amendments revised the 
    Technical Specifications (TS) 5.3.4, ``Steam and Power Conversion 
    Systems,'' and TS 15.3.7, ``Auxiliary Electrical Systems,'' to increase 
    the allowed outage times for one motor driven auxiliary feedwater pump 
    and for the standby emergency power for the Unit 1, Train B4160 Volt 
    safeguards bus (A06) from 7 to 12 days. The amendments also modified TS 
    15.3.3, ``Emergency Core Cooling System, Auxiliary Cooling Systems, Air 
    Recirculation Fan Coolers, and Contained Spray,'' to provide the 
    clarification that the service water pump (P-32E) operating with power 
    supplied by the Alternative Shutdown System is operable from offsite 
    power. The changes are one-time extensions of specific allowed outage 
    times.
        Date of issuance: September 23, 1994
        Effective date: immediately, to be implemented within 45 days
        Amendment Nos.: 153 and 157
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 19, 1994 (59 FR 
    42870) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 23, 1994.The August 
    19, 1994, submittal provided additional supplemental information that 
    did not change the initial proposed no significant hazards 
    consideration determination.No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: July 18, 1994
        Brief description of amendments: The amendments changed Technical 
    Specification 15.3.7, ``Auxiliary Electrical System'' to include the 
    allowed outage time for one of the four connected station battery 
    chargers and subsequent shutdown requirements. The amendments also 
    revised the basis for Section 15.3.7 to support the above changes.
        Date of issuance: September 29, 1994
        Effective date: immediately, to be implemented within 45 days
        Amendment Nos.: 154 and 158
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42348) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 29, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By November 14, 1994, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    MillstoneNuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: September 17, 1994
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) Surveillance Requirements 4.3.2.2, 4.6.3.1, 
    4.7.1.5.2, and 4.7.1.2.1.b by noting that surveillance requirement 
    4.0.4 is not aplicable. The amendment allows the plant to enter Modes 4 
    and 3, as necessary, to perform the required operability tests for the 
    Main Steam Isolation Valves, the engineered safety feature actuation 
    system and the turbine-driven Auxiliary Feedwater pump.
        Date of issuance: September 29, 1994
        Effective date: September 29, 1994
        Amendment No.: 96
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated September 29, 1994.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: John F. Stolz
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment:  September 18, 1994
        Brief description of amendment: The amendment modifies the 
    Technical Specifications (TS) to add a note to TS Table 3.6.3-1, 
    ``Primary Containment Isolation Valves,'' to allow operation of the 
    facility until the next plant shutdown, but not later than May 15, 
    1995, without meeting the single-failure criterion for the logic 
    circuit for containment isolation valves in the hydraulic lines 
    supplying motive force for the reactor recirculation system (RRC) flow 
    control valves.
        Date of issuance: September 29, 1994
        Effective date: September 29, 1994
        Amendment No.: 132
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications. Public comments on proposed no significant 
    hazards consideration comments received: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated September 29, 1994.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: M.H. Philips, Jr., Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502.
        NRC Project Director: Theodore R. Quay
        Dated at Rockville, Maryland, this 4th day of October 1994.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects - III/IV, Office of Nuclear 
    Reactor Regulation
    [Doc. 94-25024 Filed 10-11-94; 845 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
10/12/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
X94-11012
Dates:
September 21, 1994
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: October 12, 1994