98-28069. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 63, Number 203 (Wednesday, October 21, 1998)]
    [Notices]
    [Pages 56238-56269]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-28069]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from September 26, 1998, through October 8, 1998. 
    The last biweekly notice was published on October 7, 1998 (63 FR 
    53943).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period.
    
    [[Page 56239]]
    
    However, should circumstances change during the notice period such that 
    failure to act in a timely way would result, for example, in derating 
    or shutdown of the facility, the Commission may issue the license 
    amendment before the expiration of the 30-day notice period, provided 
    that its final determination is that the amendment involves no 
    significant hazards consideration. The final determination will 
    consider all public and State comments received before action is taken. 
    Should the Commission take this action, it will publish in the Federal 
    Register a notice of issuance and provide for opportunity for a hearing 
    after issuance. The Commission expects that the need to take this 
    action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By November 20, 1998, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: September 23, 1998.
    
    [[Page 56240]]
    
        Description of amendment request: Carolina Power & Light (CP&L) 
    proposes to revise the Harris Nuclear Plant Technical Specification 
    (TS) 3/4.6.1.3, ``Containment Air Locks,'' to clarify the requirements 
    for locking an air lock door shut. CP&L also proposes to revise TS 3/
    4.6.1.3 to be consistent with NUREG 1431, Revision 1, ``Standard 
    Technical Specifications, Westinghouse Plants,'' dated April 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        Containment Air Locks are not an accident initiating system as 
    described in the Final Safety Analysis Report [FSAR]. The proposed 
    change implements guidance for Technical Specifications associated with 
    air lock doors consistent with NUREG-1431, Revision 1, ``Standard 
    Technical Specifications, Westinghouse Plants,'' dated April 1995. 
    Additionally, clarification is provided to permit locking an inoperable 
    air lock door as required by Technical Specifications [TS]. The 
    proposed change does not affect another Structure, System, or 
    Component. The operation and design of containment air locks will not 
    be affected by this proposed change. The ability of containment to 
    mitigate an accident will not be affected by this change.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        Containment Air Locks are designed to form part of the containment 
    pressure boundary. The proposed change provides for administrative 
    controls and operating restrictions for air lock doors consistent with 
    guidance provided by the Commission. Containment Air Locks are not an 
    accident initiating system as described in the Final Safety Analysis 
    Report. The proposed change does not affect another Structure, System, 
    or Component. The operation and design of containment air locks will 
    not be affected by this proposed change.
        Therefore, the proposed change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant reduction 
    in the margin of safety.
        The proposed change to containment air locks does not affect any of 
    the parameters that relate to the margin of safety as described in the 
    Bases of the TS or the FSAR. Accordingly, NRC Acceptance Limits are not 
    affected by this change.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Pao-Tsin Kuo (Acting).
    
    Detroit Edison Company, Docket No. 50-16, Enrico Fermi Atomic Power 
    Plant, Unit 1, Monroe County, Michigan
    
        Date of amendment request: July 17, 1998 (Reference NRC-98-0044).
        Description of amendment request: The proposed amendment will 
    revise the License to allow the licensee to possess special nuclear 
    material in a quantity totaling no more than 15 grams of uranium-235, 
    uranium-233, or plutonium, or any combination thereof and with 
    plutonium totaling no more than 2 curies.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration using the standards in 10 CFR 50.92(c). The licensee's 
    analysis is presented below:
        (1) Does the proposed change significantly increase the probability 
    or consequences of an accident previously evaluated?
        The proposed changes do not involve a significant increase in the 
    probability or consequences of an accident. Possessing trace amounts of 
    special nuclear material cannot affect the probability of the analyzed 
    sodium or liquid waste accidents. The ability to possess such material 
    does not itself change any methods of handling liquid waste or sodium. 
    Possession of special nuclear material could potentially increase the 
    consequences of an accident if it was in use or in the vicinity if an 
    accident occurs. However, the increase in consequences would not be 
    significant due to the limitations on radioactivity content of such 
    special nuclear material. The special nuclear material limit is below 
    that requiring an emergency plan or maximum dose evaluation per 10 CFR 
    70.22(i). Since the quantity is below that requiring an offsite 
    emergency plan or evaluation, even if all the special nuclear material 
    allowed to be possessed by the proposed amendment were released during 
    a postulated accident, the consequences would not be significantly 
    increased. If the provision allowing for possession of more than 15 
    grams of special nuclear material or 2 curies of plutonium were to be 
    used in the future due to identified plant contamination, the 
    requirements of 10 CFR 70.22(i) would need to be assessed and a dose 
    evaluation performed or an emergency plan submitted if required to 
    ensure the analyzed accident is appropriately addressed and mitigated. 
    Any such special nuclear material would be contained in the remaining 
    plant contamination, since fuel and blanket material were shipped 
    offsite during 1973-1975. Therefore, this amendment does not involve a 
    significant increase in the probability or consequences of an accident.
        (2) Will the proposed amendment create the possibility of a new or 
    different kind of accident from any accident previously analyzed?
        The proposed changes do not create the possibility of a new or 
    different type of accident from any previously evaluated. Allowing 
    possession of small amounts of special nuclear material does not change 
    methods of monitoring the facility or operations or surveillance of any 
    systems at Fermi 1. The amount requested is below that requiring 
    criticality monitoring per 10 CFR 70.24, and the separation of the 
    special nuclear material will not be permitted. Thus, there is no 
    identified physical mechanism for creating an accident based on the 
    existence of such material in the quantities specified. If the 
    provision allowing for possession of more than 15 grams of special 
    nuclear material or 2 curies of plutonium if is identified in plant 
    contamination in the future were to be invoked, applicable provisions 
    to ensure public safety per 10 CFR Part 70, Part 73, and Part 74 will 
    apply. For these reasons, allowing Detroit Edison to possess very 
    limited amounts of special nuclear material at Fermi 1 will not create 
    the possibility of a new or different type of accident.
    
    [[Page 56241]]
    
        (3) Will the proposed change significantly reduce the margin of 
    safety at the facility?
        The proposed changes do not involve a significant reduction in the 
    margin of safety at Fermi 1. No changes to any systems, or the status 
    of any systems or structures, are created by this amendment. Being able 
    to have a very limited amount of special nuclear material at Fermi 1 
    will not significantly reduce the margin of safety because a 10 CFR 
    Part 20 program is already in place, and the amount of special nuclear 
    material is being limited below criteria requiring an emergency plan, 
    special nuclear material control program, or criticality monitoring. If 
    more than 15 grams of special nuclear material or 2 curies of plutonium 
    is identified in plant contamination in the future, the proposed 
    license amendment will require the applicable portions of 10 CFR Part 
    70, Part 73, and Part 74 to apply for the amount identified. For these 
    reasons, this amendment will not significantly reduce the margin of 
    safety at Fermi 1.
        NRC staff has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
        Attorney for licensee: John Flynn, Esquire, Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Branch Chief: John W.N. Hickey.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: April 30, 1998.
        Description of amendment request: Arkansas Nuclear One--Unit 2 
    (ANO-2) Technical Specification (TS) 4.8.1.1.2.c.3 has been revised to 
    relocate the specific value for the single largest post-accident load 
    to the Bases associated with TS 4.8. The revised TS 4.8.1.1.2.c.3 would 
    require the licensee to verify the generator capability to reject a 
    load greater than or equal to its associated single largest post-
    accident load.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The Diesel Generators (DGs) are not identified as the initiator of 
    any accident previously analyzed. The design and function of the DGs 
    are unaffected by this proposed change. Applying more restrictive 
    acceptance criterion to the single largest load rejection test can not 
    result in an increase in the probability of accidents previously 
    evaluated and will provide increased assurance that the DGs will 
    perform as intended to support the mitigation of accidents previously 
    evaluated.
        Therefore, this change does not involve a significant increase in 
    the probability or consequences of any accident previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed change corrects information contained in the technical 
    specification and does not involve any design change, plant 
    modification, change in analyzed DG performance, or change in plant 
    operation. Since the DGs are not considered to be event initiators, 
    their accident mitigation function is unaffected, and normal operation 
    is unaffected, the proposed change does not result in new or different 
    accidents from those previously analyzed.
        Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The design and function of the DGs are unaffected by the proposed 
    change. Applying more restrictive acceptance criterion to the single 
    largest load rejection test will provide increased assurance that the 
    DGs will perform as intended to support the mitigation of postulated 
    accidents. DG performance is proposed to meet a more stringent 
    standard.
        Therefore, this change does not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: May 18, 1998.
        Description of amendment request: The proposed changes delete the 
    ANO-2 TS 3.6.2.2 and 4.6.2.2 requirements, and their associated bases, 
    for the sodium hydroxide addition system and add new limiting 
    conditions for operation, action statements, surveillance requirements, 
    and bases information for trisodium phosphate baskets which will be 
    installed during the next ANO-2 refueling outage (2R13). The capability 
    to add sodium hydroxide to the containment spray system during the 
    initial phase of a loss-of-coolant accident will be replaced with 
    crystalline trisodium phosphate (TSP) dodecahydrate stored in 
    containers located on the floor of the containment building.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change modifies the method of containment spray sump 
    pH control. The containment spray function is important for containment 
    heat removal/pressure mitigation. However, this change does not affect 
    the probability of occurrence of the accident initiators which result 
    in the need for containment heat removal and pressure mitigation. Since 
    the TSP baskets are seismically mounted passive devices located inside 
    the containment, they cannot initiate a transient or affect the 
    probability of occurrence of any previously analyzed accident.
        The proposed change only modifies the chemical composition of the 
    containment spray and sump fluid. The proposed changes do not affect 
    the heat removal/pressure mitigation functions of the system since the 
    spray flow rate and droplet size are unchanged. The proposed change 
    also will not adversely affect the radiological doses for the design 
    basis accident (DBA) loss-of-coolant accident (LOCA) at the exclusion 
    area boundary, low
    
    [[Page 56242]]
    
    population zone, control room, or emergency response facility. The 
    change does not adversely affect the calculated peak clad temperature 
    for the DBA LOCA or the environmental qualification (EQ) of components 
    located inside containment.
        Therefore, this change does not involve a significant increase in 
    the probability or consequences of any accident previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed change allows the use of TSP as a buffering agent for 
    the containment sump instead of sodium hydroxide (NaOH) added via the 
    containment spray system. The TSP baskets are passive devices that have 
    minimal impact on any other system except through water chemistry. The 
    change in water chemistry does not adversely affect any safety system 
    or required safety functions. The replacement of NaOH additive with TSP 
    will not change the probability of a malfunction of safety-related 
    equipment.
        Potential malfunctions relating to the proposed modification have 
    been evaluated for their effect on plant safety and have been found to 
    be non-significant. Additionally, the transient pH behavior of the 
    containment spray flow does not adversely affect the EQ of components 
    located inside containment.
        Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The proposed change does not adversely affect the ability of the 
    containment spray system to perform the functions of containment heat 
    removal, pressure mitigation, and fission product (iodine) retention. 
    The proposed change does not adversely affect any equipment credited in 
    the safety analysis. Also, the proposed change does not increase the 
    peak clad temperature or the offsite doses due to the DBA LOCA.
        Therefore, this change does not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: June 29, 1998.
        Description of amendment request: The proposed amendment would 
    revise the as-found lift setting tolerance for the ANO-2 main steam 
    safety valves (MSSVs) and pressurizer safety valves (PSVs) will be 
    increased. The proposed increase in the lift setting tolerance is 
    contingent upon a reduction in a linear power level-high setpoint and 
    use of the latest small break loss of coolant accident (SBLOCA) 
    methodology for development of the Core Operating Limits Report (COLR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        This change allows for a larger 3% tolerance versus 
    1%, -3% as-found lift setting tolerance. The proposed 
    change does not involve any change to the physical characteristics of 
    the main steam safety valves (MSSVs) and pressurizer safety valves 
    (PSVs), and will have no impact on the as-left settings. During 
    testing, the MSSVs and PSVs will continue to adjusted to 1% 
    of the Technical Specification (TS) lift setting.
        The impact on the Safety Analysis Report (SAR) analyses when the 
    as-found lift setting tolerances are increased has been evaluated and 
    the effects upon the impacted events have been found to be within 
    acceptable limits, providing the allowable linear power level with 
    three inoperable MSSVs is revised from 45% to 36%, and that the latest 
    NRC approved C-E small break loss of coolant analysis (LOCA) evaluation 
    model, CENPD-137, Supplement 2-P-A, is included as a methodology for 
    determination of operating parameters identified within the core 
    operating limits report (COLR). With these concurrent changes, plant 
    systems required for safe operation and shutdown will continue to be 
    available to fulfill their safety function as described in the SAR. 
    Steam production in excess of relief capacity is precluded by the 
    physical design of the plant and operation of the reactor protection 
    system. Revision of the MSSV as-found lift setting tolerance from 
    1%, 3% to 3% does not alter safety 
    analyses conclusions.
        Therefore, this change does not involve a significant increase in 
    the probability or consequences of any accident previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        This change does not create any new plant configuration or 
    operational mode. This proposal to increase the MSSV and PSV as-found 
    lift setting tolerance does not modify equipment or change the manner 
    in which the MSSVs and PSVs will be operated. ASME design requirements 
    for maintaining system operating pressure limits below the maximum 
    design pressure of 1210 psia for plant secondary systems, and 2750 psia 
    for the reactor coolant system (RCS) are not impacted. The reduction in 
    allowable linear power level when three MSSVs are inoperable assures 
    plant operation within current analysis assumptions. The addition of 
    topical report CENPD-137, Supplement 2-P-A, as a reference to develop 
    the COLR is bounded by assumptions within the existing safety analysis. 
    The cycle specific COLR analyses will continue to be performed 
    utilizing NRC approved methodologies. The TS changes do not require any 
    new equipment be included in the design basis, and current equipment 
    will continue to be operated in a manner consistent with its design.
        Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The upper tolerance limit for design pressure is not affected by 
    this change. During the most severe anticipated operational transient, 
    the Secondary System pressure and RCS pressure will not exceed 110% of 
    design pressure. The MSSV and PSV lift settings will continue to be set 
    within -1% of the TS lift setting during surveillance testing.
        The decrease in the peak cladding temperature of the reactor fuel, 
    due to a change in the methodology for analysis, does not significantly 
    impact previous analytical results. The current and previous analytical 
    methodologies are approved by the Staff.
        The impact of the proposed changes on the ANO-2 SAR analyses have 
    been evaluated. The evaluation demonstrates that the results of the 
    impacted events
    
    [[Page 56243]]
    
    remained within the acceptable limits providing the maximum linear 
    power level percentage for three inoperable MSSVs is reduced. This 
    reduction in maximum allowable linear power level assures that adequate 
    steam relief capacity will be available to prevent overpressurizing the 
    secondary steam system during the most severe anticipated operational 
    transient.
        Addition of topical report CENPD-137, Supplement 2-P-A, will not 
    reduce the existing TS operability and surveillance requirements. The 
    cycle specific COLR limits for future reloads will continue to be 
    developed based on NRC-approved methodologies. The ANO-2 TSs will 
    continue to require that the core be operated within these limits.
        The cumulative impact of all of the proposed changes and the 
    results of the impacted events have been found to be within acceptable 
    limits. The system capabilities to mitigate and/or prevent accidents 
    will be the same as they were prior to these changes.
        Therefore, this change does not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: June 29, 1998.
        Description of amendment request: These proposed changes are in 
    Technical Specification 3.4.2, ``Reactor Coolant System--Safety 
    Valves--Shutdown,'' and Technical Specification 3.4.12, ``Reactor 
    Coolant System--Overpressure Protection'' regarding the low temperature 
    overpressure protection system. The specific changes include modifying 
    the requirements for the pressurizer code safety valve requirements 
    specified by Technical Specification 3.4.2 and a modification of the 
    safety injection tank isolation requirements specified in Technical 
    Specification 3.4.12.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The reactor coolant system (RCS) is designed with overpressure 
    protection devices to be used in all modes of operation. The changes to 
    Technical specification (TS) 3.4.2 will ensure that, if no pressurizer 
    code safety valves are operable, the RCS will be cooled down to the 
    mode of applicability of the low temperature overpressure protection 
    (LTOP) system (TS 3.4.12) within 12 hours. The LTOP relief valves 
    provide sufficient relief capacity to protect the RCS from 
    overpressurization when the RCS inlet temperature (Tc) less 
    than or equal to 220 deg. F. Therefore, this change will ensure the 
    proper actions will be taken that will ensure adequate overpressure 
    protection of the RCS. These actions are not accident initiators, and 
    therefore do not involve a significant increase in the probability of 
    any accident previously evaluated.
        The proposed change to TS 3.4.12 provides additional operational 
    flexibility for the use of the safety injection tanks (SITs) as an 
    additional inventory source during Modes 4, 5, and 6 when the RCS is in 
    LTOP conditions. The ability to use the SITs, with a pressure less than 
    300 psig is within the existing LTOP analysis. The LTOP analysis 
    ensures that under the analyzed worst case overpressurization event, 
    the RCS is protected. The 300 psig SIT pressure limit, corrected for 
    instrument uncertainty, will prevent a challenge to the LTOP relief 
    valves and therefore the RCS will be assured of overpressure 
    protection. The SIT pressure limit will also be low enough to prevent 
    an inadvertent isolation of the shutdown cooling system and thus 
    prevent a loss of shutdown cooling due to placing an SIT in service. 
    The remaining changes included in this amendment request are considered 
    administrative in nature and are therefore considered acceptable.
        Based on the above discussions, these changes do not involve a 
    significant increase in the probability or consequences of any accident 
    previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed changes included in this amendment request provide 
    additional operational flexibility for the use of the SITs and specify 
    the proper actions to be taken that will ensure adequate overpressure 
    protection of the RCS. The LTOP relief valves have already been 
    evaluated for operation below 220 deg. F. The changes do not introduce 
    any new plant configurations. No new accident possibilities are being 
    introduced by these changes. Therefore, the proposed changes do not 
    create the possibility of a new or different kind of accident from any 
    previously evaluated.
        3. Does Not involve a significant reduction in the margin of 
    safety.
        The proposed change to the TS 3.4.2 action statement requires the 
    Tc be less than or equal to 220 deg. F when no pressurizer 
    code safety valves are available. When Tc is less than or equal to 
    220 deg. F, the LTOP system operability is required by TS 3.4.12. This 
    action will provide assurance that the RCS will be protected from an 
    overpressurization event and therefore increases the margin of safety.
        The requirements to maintain one pressurizer code safety valve in 
    Mode 4 when Tc is less than or equal to 220 deg. F and in 
    Mode 5 has been removed by the proposed revision to TS 3.4.2. The LTOPs 
    provide adequate RCS over pressure protection during these modes 
    without reliance on the pressurizer code safeties. Maintaining the 
    requirement to require one pressurizer code safety to be operable at 
    the same time as the LTOP system is required to be operable, provides 
    no additional plant safety. An operable LTOP system prevents RCS 
    pressure from increasing high enough to challenge the pressurizer code 
    safety lift setpoints.
        The current TS 3.4.12 LTOP limits are based on an analysis that 
    uses the methodology outlined in the ASME Code Case N-514. This code 
    case defines the margin of safety for the current LTOP limits. This 
    code case was utilized in the development of TS 3.4.12. The safety 
    factor utilized by the code case provides a reasonable vessel 
    overpressure allowance for conditions expected during a low temperature 
    transient. The margin of safety is not reduced with SITs in service and 
    pressurized to less than 300 psig because this condition is bounded by 
    the existing LTOP analysis. Therefore, this change does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
    [[Page 56244]]
    
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: June 29, 1998.
        Description of amendment request: The proposed change to the 
    Arkansas Nuclear One Unit 2 Technical Specifications would provide a 
    range of acceptable values for the 4160 Volt bus loss of voltage 
    values. The present Technical Specification Table 3.3-4, item 7.a 
    provides a single value for both the trip and the allowable values for 
    the 4160 Volt bus loss of voltage requirements. These table entries do 
    not include an acceptable range or an explicit indication of the 
    allowed tolerance that the actual setting is allowed to vary from the 
    indicated value. The proposed change replaces the specific trip value 
    with an explicit range of acceptable allowable values.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The two 4160 Volt (V) vital bus loss of voltage protection relays 
    that are provided on each of the 4160 V safety buses are provided to 
    detect loss of voltage, isolate the safety buses, initiate load 
    shedding, and start the associated emergency diesel generator. This 
    safety function is unchanged by the proposed setpoint revisions. The 
    revised settings for the loss of voltage protection relays will 
    continue to provide the safety function with no appreciable additional 
    time delay. The proposed time delays are within those assumed in the 
    ANO-2 safety analyses. Additionally, the lower voltage settings will 
    prevent unnecessary isolations from the off-site power sources which 
    will contribute to reducing the probability of a loss of off-site power 
    due to off-site power system transients.
        The ANO-2 technical specifications will continue to require the 
    4160 V loss of voltage functions to be surveillance tested at their 
    present frequency without changing the modes in which the surveillance 
    is required or the modes of applicability for these components. The 
    technical specifications will continue to require the same actions as 
    currently exist for the inoperability of one or more of the 4160 V loss 
    of voltage channels. Therefore, this change does not involve a 
    significant increase in the probability or consequences of any accident 
    previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed change introduces no new modes of plant operation or 
    new plant configuration. The 4160 V vital bus loss of voltage 
    protection relays are required to operate following a complete loss of 
    off-site power to initiate the bus power source transfer to on-site 
    power, i.e., the emergency diesel generators, to prevent a loss of all 
    AC power. This safety function is unchanged by the proposed setpoint 
    revisions, and the proposed setpoints continue to provide the required 
    actions consistent with the ANO-2 safety analysis. Therefore, this 
    change does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The two undervoltage relays located on each 4160 V safety bus are 
    provided to detect loss of voltage, isolate the safety buses, initiate 
    load shedding, and start the emergency diesel generators. This safety 
    function is unchanged by the proposed setpoint revisions.
        The lower loss of voltage values do not affect the safety function 
    since there is no appreciable time difference in reaching the lower 
    setpoints during a loss of voltage event. The maximum proposed time 
    delay setting with the minimum loss of voltage relay setting is within 
    those used in the ANO-2 safety analysis. The revised settings for the 
    relays will continue to provide the safety function with no appreciable 
    additional time delay.
        Removal of the trip value from the technical specifications is 
    consistent with that which is presented in NUREG-1432, ``Standard 
    Technical Specifications for Combustion Engineering Plants.'' The 
    current ANO-2 technical specifications and NUREG-1432 both indicate 
    that if the setpoint is outside the allowable value column, the 
    associated channel is declared inoperable. This approach is consistent 
    with this proposed technical specification change.
        The trip and allowable values listed in the technical 
    specifications for the loss of voltage protection for the 4160 V buses 
    are presently the same. With these values being the same, if the trip 
    value is exceeded, the allowable value will also be exceeded. This 
    change provides a range of acceptable allowable values for these 
    relays. By relocating the trip values in the surveillance test 
    procedures, the procedural limits for the voltage and time delay 
    settings can be adjusted to ensure margin to the allowable values. 
    Additionally, the lower voltage settings will help to prevent 
    unnecessary isolation from the off-site power sources due to off-site 
    perturbations in the electrical grid, and thus contribute to increasing 
    the margin of safety. Therefore, this change does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: June 29, 1998.
        Description of amendment request: The proposed Technical 
    Specification change revises the surveillance testing requirements for 
    the Arkansas Nuclear One--Unit 2 (ANO-2) direct current (DC) electrical 
    distribution system. ANO-2 is planning on modifying the 120 volt vital 
    alternating current (AC) electrical distribution system by installing 
    new inverters during the next scheduled refueling outage (2R13). This 
    modification will increase the normal 125 volt vital DC system loads by 
    adding the inverters as a normal load. The power for each 125 volt 
    vital DC system is normally supplied by its associated battery charger. 
    ANO-2 is in the process of replacing the vital DC battery chargers by 
    plant modification to ensure all the battery chargers are of sufficient 
    capacity to provide the necessary current requirements for the normal 
    125 volt vital DC loads. The proposed change to specification 
    4.8.2.3.c.4 is required to ensure the new chargers are adequately 
    tested to support the associated inverter replacement.
    
    [[Page 56245]]
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Technical Specification (TS) surveillance requirement (SR) 
    4.8.2.3.b.2 requires the battery banks for each of the vital 125 volt 
    direct current (DC) systems to be inspected to ensure that no visible 
    corrosion exists at the terminals or the connectors. This SR has been 
    modified to allow the present corrosion inspection, or the measurement 
    of the resistance of the associated battery connections. The resistance 
    measurement provides an indication of physical damage or abnormal 
    deterioration that could potentially degrade battery performance and 
    has been an accepted alternative to the visual inspection requirement.
        The Bases change associated with TS 3.8.2.3 Action ``b'' is 
    considered administrative in nature and simply clarifies the intent of 
    the action without changing the requirements of the action or its 
    required completion time. The station batteries are not classified as 
    accident initiators in the ANO-2 accident analysis. The 125 volt class 
    1E batteries are credited for accident mitigation in the accident 
    analysis. The above described changes do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        Each battery charger is required to have sufficient capacity to 
    restore the battery from the design minimum charge to its fully charged 
    state while supplying normal steady state loads. The minimum specified 
    TS surveillance required charger amperage limit will ensure this 
    capacity. The additional charger output is presently accounted for in 
    the emergency diesel generator loading tables in the Safety Analysis 
    Report (SAR). Loss of one train of the vital 125 volt DC system is an 
    accident that has been evaluated in the SAR. The capacity of the 
    battery chargers is not a factor in the probability of this accident 
    occurring. Therefore, the changes associated with this technical 
    specification amendment request do not increase the probability of any 
    accident previously evaluated.
        The proposed technical specification changes do not modify the 
    limiting condition for operation or the associated action statements 
    regarding operability of the battery chargers other than clarifying 
    these requirements. The frequency at which the battery charger 
    operability is demonstrated by surveillance testing is not being 
    modified by this technical specification change request. The proposed 
    battery charger surveillance testing acceptance criterion will more 
    appropriately demonstrate the capability of this equipment. This change 
    does not affect the consequences of any of the previously evaluated 
    accidents.
        Therefore, this change does not involve a significant increase in 
    the probability or consequences of any accident previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        Technical specification SR 4.8.2.3.b.2 requires the battery banks 
    for each of the 125 volt systems to be inspected to ensure that no 
    visible corrosion exists at the terminals or the connectors. This SR 
    has been modified to allow the present corrosion inspection, or to 
    perform resistance readings on the associated battery connections. The 
    visual inspection is required to detect corrosion of the battery 
    connections. The resistance measurement of the associated battery 
    connections provides an acceptable alternative to the visual inspection 
    requirement and provides an indication of physical damage or abnormal 
    deterioration that could potentially degrade battery performance.
        The availability of an extra battery charger for each train 
    following the plant modification provides a more reliable configuration 
    without introduction of any new modes of plant operation. No new 
    accident possibilities are being introduced by the proposed change to 
    the surveillance testing specification for battery charger amperage. 
    Increasing the surveillance testing amperage limit for the battery 
    chargers does not create the potential for any different accident since 
    the new value remains within the design capacity of the components.
        Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        TS SR 4.8.2.3.b.2 has been modified to allow resistance readings on 
    the associated battery connections or the performance of the present 
    visual inspection requirements. The resistance measurement of the 
    associated battery connections provides an acceptable alternative to 
    the visual inspection requirement and provides an indication of 
    physical damage or abnormal deterioration that could potentially 
    degrade battery performance without a significant reduction in the 
    margin of safety.
        The proposed technical specification surveillance requirements for 
    the battery chargers continues to require testing of battery chargers 
    at the present duration and frequency. These requirements will also 
    apply to the second charger being installed for each Class 1E battery 
    train. Each of the new battery chargers has sufficient capacity to 
    restore the battery from the design minimum charge to its fully charged 
    state while supplying normal steady state loads. The proposed 
    surveillance specification change does not involve a significant 
    reduction in the margin to safety since the demonstrated capacity will 
    be of a higher amperage requirement than is demonstrated during the 
    surveillance test with the existing configuration. Increasing the 
    required amperage value assures the surveillance test will continue to 
    demonstrate the chargers can provide significantly more current than is 
    necessary to meet the design requirements. Therefore, this change does 
    not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: August 6, 1998.
        Description of amendment request: The proposed technical 
    specification change revises the Action requirements for the Arkansas 
    Nuclear One--Unit 2 (ANO-2) Control Element Assembly (CEA) position 
    indicator channels. The Action requirements listed in Specification 
    3.1.3.2 are being modified consistent with the requirements of NUREG-
    1432, ``Standard Technical Specifications for Combustion Engineering 
    Plants.'' The proposed changes also include the relocation of Technical 
    Specification Table 3.8-1, ``Containment Penetration Conductor 
    Overcurrent Protective Devices'' per
    
    [[Page 56246]]
    
    NRC Generic Letter 91-08, ``Removal of Component Lists From Technical 
    Specifications.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        This technical specification (TS) change request contains the 
    relocation of Table 3.8-1, Containment Penetration Conductor 
    Overcurrent Protective Devices, and changes to the control element 
    assembly (CEA) position indication.
        Generic Letter (GL) 91-08, ``Removal of Component Lists From 
    Technical Specifications,'' was issued as a TS line item improvement by 
    the NRC. Table 3.8-1 is one of the specific lists of components 
    contained in the GL. TS Table 3.8-1 and all its references have been 
    removed from Specification 3/4.8.2.5 in accordance with the GL. This 
    change is considered administrative in nature because the requirements 
    for operability, the limiting conditions for operation, the 
    surveillance requirements and their frequencies for the containment 
    penetration conductor overcurrent protective devices remains the same. 
    This amendment request fundamentally modifies the physical location of 
    the devices listed in Table 3.8-1 from the TS to the plant procedures. 
    These changes have no affect on the probability or consequences of any 
    accident previously evaluated.
        The remaining changes included in this amendment request are those 
    relating to the CEA position indication. The Action requirements for TS 
    3.1.3.2 were modified to be consistent with the requirements of NUREG-
    1432, ``Standard Technical Specifications for Combustion Engineering 
    Plants.'' The most recent revision of NUREG-1432 was used to produce 
    this change because it represents the latest guidance for the TS CEA 
    position indication requirements that are applicable to ANO-2 and 
    acceptable to the NRC.
        The requirement was removed from TS 3.1.3.2 that restricted each 
    CEA group to a maximum of one CEA with less than two of the required 
    position indicator channels. NUREG-1432 places no requirements on the 
    number of CEAs in a group with less than two of the required position 
    indicator channels. NUREG-1432 would allow all the CEAs in a group to 
    have only one of the required CEA position indications operable. In 
    this situation, the associated CEAs with less than two of the required 
    position indicator channels would have to be placed at their ``Full 
    In'' or ``Full Out'' limits.
        TS 3.1.3.2 was modified to allow the use of the ``Full In'' or 
    ``Full Out'' limits which ensures this specification is consistent with 
    its bases and NUREG-1432. The TS will still maintain the requirements 
    for two independent means of determining CEA position with this 
    amendment request. With two independent means of determining CEA 
    position, reliable determination of actual CEA position will be 
    maintained.
        Additionally, NUREG-1432 does not require the placement of any 
    other CEAs in the associated group at the ``Full Out'' limit when one 
    of the CEAs in the group has only one of the required position 
    indication systems operable. All of the remaining CEAs in the 
    associated group still have at least two independent means of CEA 
    position indication or they would already be required to be positioned 
    to the ``Full Out'' limit to restore the second position indication. 
    The TS retains the requirements for the individual and group CEA 
    alignment in accordance with Specifications 3.1.3.1 and 3.1.3.6. These 
    requirements also eliminate the need for pulling the remaining CEAs in 
    the group to the ``Full Out'' limit as long as the alignment 
    requirements are maintained.
        These changes will allow the operator more time to focus on the 
    individual CEA position indication problem rather than moving the 
    remainder of the CEAs in the group unnecessarily. Anytime that a CEA is 
    moved, a small probability exists for it to slip or drop into the core. 
    If this were to occur while attempting to align the group to the ``Full 
    Out'' limit, a reactor transient would be initiated. Additionally, 
    anytime the CEAs are operated, a small probability of an error exists. 
    Removing the unnecessary requirement for the group withdrawal could 
    decrease the probability of CEA misoperation. CEA position indication 
    is not considered as an accident initiator. Retaining the requirements 
    to maintain at least two independent means of determining CEA position 
    will ensure the consequences of all the accidents previously evaluated 
    remain unchanged.
        Therefore, this change does not involve a significant increase in 
    the probability or consequences of any accident previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The portions of this change that are made in accordance with GL 91-
    08 are considered administrative in nature and do not result in the 
    creation of a new or different kind of accident from any previously 
    evaluated.
        The bases for TS 3.1.3.2 state that the action statements 
    applicable to inoperable CEA position indicators permit continued 
    operation when the positions of CEAs with inoperable position 
    indicators can be verified by the ``Full In'' or ``Full Out'' limits. 
    Although TS 3.1.3.2 may have originally been intended to allow 
    continued operation using the ``Full In'' limits, it has never been 
    clearly addressed in the specification. NUREG-1432 allows the use of 
    both the ``Full In'' or ``Full Out'' limits. This amendment request 
    will not change the methods for CEA operation, although it will reduce 
    unnecessary CEA manipulations due to CEA position indication problems.
        The requirements of Specification 3.1.3.1 will ensure that an 
    individual CEA is maintained in proper alignment with the remaining 
    CEAs in the group. Specification 3.1.3.6 will ensure the CEA groups are 
    maintained within the proper withdrawal sequence and insertion limits. 
    Specification 3.1.3.5 will ensure the shutdown CEA groups are 
    maintained in the ``Full Out'' position. The CEA position indication 
    changes allowed by this amendment request, including the allowance to 
    use the ``Full In'' limits, can produce a CEA configuration that is 
    different from that allowed by the current TSs. However, the allowed 
    configurations will be bounded by the TS 3.1.3.2 Action ``c'' 
    requirements for compliance with Specifications 3.1.3.1, 3.1.3.5, and 
    3.1.3.6. Therefore, the action requirements of TS 3.1.3.2 will ensure 
    the CEAs are operated consistent with the safety analysis assumptions.
        Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The portions of this change that are made in accordance with GL 91-
    08 are considered administrative in nature and have no effect on the 
    margin of safety. The remaining changes can result in a lower 
    probability of CEA misoperation and reduce the potential of plant 
    transients due to CEAs that slip or drop into the core while performing 
    unnecessary group realignments. These changes can also reduce 
    unnecessary plant shutdowns, due to unneeded restrictions on CEA 
    position indication. An unnecessary plant shutdown produces an 
    opportunity for plant
    
    [[Page 56247]]
    
    upsets that can be avoided by this change. The proposed TS provide an 
    equivalent level of safety as those specifications that currently 
    exist. Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: September 17, 1998.
        Description of amendment request: The proposed amendment addresses 
    a problem associated with the existing technical specifications being 
    inconsistent with the design of the plant protection system (PPS). The 
    PPS uses a design in which a single bistable is used to automatically 
    enable the selected core protection calculator (CPC) trip functions 
    whenever a permissive exists to bypass the high logarithmic power level 
    trip function. The technical specifications allow the bypass of the 
    high logarithmic power trip when power is above 10-4 percent 
    power and allow bypasses of the affected CPC trips when power is below 
    10-4 percent power. The proposed technical specification 
    change establishes a range for the bistable setpoint to be within such 
    that it is possible to meet both of its design functions while also 
    meeting the technical specification requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        This technical specification (TS) change request modifies the power 
    level at which two of the three operating bypasses can be set to 
    operate. This change is necessary because the present plant bistable 
    design requires a range for this bistable to operate within rather than 
    a specific setpoint as required by the present TS. The single bistable 
    associated with these operating bypasses is designed with an inherent 
    hysteresis loop and therefore requires an operating range. The band of 
    10-4% to 10-2% of rated thermal power provides 
    the bistable an adequate operating range to account for the inherent 
    bistable hysteresis, allow for bistable drift, and provides margin for 
    the applicable uncertainties. Regardless of the actual bistable 
    setpoint within this band, the bistable design ensures that either the 
    high logarithmic power level or the core protection calculator (CPC) 
    generated trips are available to provide reactor trip protection. The 
    CPC and logarithmic power operating bypasses and their setpoints are 
    not considered credible accident initiators and therefore modifying 
    their setpoints does not involve a significant increase in the 
    probability of an accident previously evaluated.
        The automatic removal function of these operating bypasses is 
    designed to mitigate the consequences of accidents. As described within 
    the background section of the TS change request, the safety analyses 
    associated with operating bypasses have been reviewed for the 
    acceptability of these changes. This review concluded that these 
    changes are considered bounded by the existing safety analyses. Since 
    these TS changes are bounded within the present safety analyses, they 
    do not involve a significant increase in the consequences of an 
    accident previously evaluated.
        The remaining changes included in this TS change request are being 
    made to clarify the existing requirements for the operating bypasses 
    and to establish consistency with the above described changes. The 
    remaining changes have been found acceptable because they are 
    considered administrative in nature and have no effect on the 
    probability or consequences of an accident previously evaluated.
        Therefore, this change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. Does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        There are no physical plant modifications being made to the plant 
    as a result of this change. The only function that is required by the 
    TS and modified by this change is associated with the allowed setpoint 
    for the automatic bypass removal feature of the CPCs. This feature will 
    still be required by the TS, but will be allowed a slightly higher 
    setpoint. The system connections and the reactor trip setpoints are not 
    affected by this change. The CPC and logarithmic power operating 
    bypasses and their setpoints are not considered as credible accident 
    initiators. Therefore, this change does not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The safety analyses associated with these operating bypasses have 
    been reviewed for the acceptability of these changes. This review 
    concluded that the changes associated with this TS change request are 
    considered bounded within the existing safety analyses. The associated 
    safety analyses have been considered to be acceptable because they have 
    produced acceptable results and thus provide an acceptable margin to 
    safety. Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: June 29, 1998.
        Description of amendment request: The proposed changes modify 
    Technical Specification (TS) 3.7.6.1 (Control Room Emergency Air 
    Filtration System--Modes 1-4), TS 3.7.6.2 (Control Room Emergency Air 
    Filtration System--Modes 5 and 6), TS 3.7.6.3 (Control Room Air 
    Temperature--Modes 1-4), TS 3.7.6.4 (Control Room Air Temperature--
    Modes 5 & 6), and TS 3.7.6.5 (Control Room Isolation and 
    Pressurization), and the associated Bases.
        The proposed changes to the control room ventilation TS affects the 
    Applicability and the Actions. These changes will make the TS 
    consistent with NUREG-1432 (Standard Technical Specifications 
    Combustion Engineering
    
    [[Page 56248]]
    
    Plants), as applicable, and the accident analysis. The proposed changes 
    to the TS Bases make the Bases consistent with the TS and also clarify 
    that suspending movement of irradiated fuel assemblies shall not 
    preclude movement to a safe conservative position.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this proposed 
    change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The proposed changes revise the control room ventilation Technical 
    Specifications (TS) Actions to delete the Action statement to suspend 
    all operations involving positive reactivity changes, and adds an 
    Applicability and Action related to the movement of irradiated fuel 
    assemblies. The changes also add an Applicability footnote and revise 
    the Bases to allow irradiated fuel assemblies to be placed in a safe 
    conservative position when movement is required to be suspended. Other 
    changes to the Bases are being made to be consistent with the TS. These 
    changes do not affect the probability of an accident. The control room 
    ventilation systems (ventilation, temperature, or envelope) do not 
    affect the initiators of an accident; therefore, the changes do not 
    alter the initiators of any analyzed events.
        The administrative and more restrictive changes do not affect the 
    consequences of an accident. The administrative changes add an 
    Applicability footnote and revise the TS Bases to make them consistent 
    with the TS. This will ensure the applicable control room ventilation 
    system TS are entered during movement of irradiated fuel assemblies and 
    that there is no confusion associated with the Bases being 
    inconsistent. The more restrictive change of adding the Applicability 
    during movement of irradiated fuel assemblies and the Action to suspend 
    movement of irradiated fuel assemblies eliminates the precursor to the 
    fuel handling accident which prevents the fuel handling accident from 
    occurring when the control room ventilation systems are inoperable. The 
    addition of this Action ensures the event that may release 
    radioactivity is precluded when the control room ventilation systems 
    are inoperable.
        The less restrictive changes (deleting the requirement to suspend 
    positive reactivity changes and a Bases change which allows irradiated 
    fuel assemblies to be placed in a safe conservative position when 
    movement has been suspended) do not affect the consequences of an 
    accident because no accident mitigator is affected. The safety analysis 
    credits instrumentation to detect a boron dilution accident and alert 
    the control room staff. After the control room staff is alerted, the 
    accident is terminated without a radioactive consequence. These 
    instruments are required to be Operable and if one is inoperable, 
    positive reactivity changes are required to be suspended. If both 
    instruments become inoperable, along with suspension of positive 
    reactivity additions, boron concentration is required to be determined 
    at frequencies specified in the Core Operating Limits Report (only when 
    source range neutron flux monitors are inoperable). Also, the shutdown 
    margin (SDM) is required to be met. If the SDM requirements are not 
    met, action must be taken to borate (addition of negative reactivity) 
    until the SDM is restored. Therefore, if the control room ventilation 
    systems are inoperable, suspension of positive reactivity changes are 
    not required. The added statement in the Bases allows irradiated fuel 
    assemblies to be placed in a safe conservative position to preclude a 
    fuel handling accident from occurring. These Actions ensure that 
    appropriate measures are taken to preclude events that would require 
    the control room to be isolated when any of the control room 
    ventilation systems are inoperable.
        Therefore, the proposed changes will not involve a significant 
    increase in the probability or consequences of any accident previously 
    evaluated.
        2. Will operation of the facility in accordance with this proposed 
    change create the possibility of a new or different type of accident 
    from any accident previously evaluated?
        Response: No.
        The proposed changes revise the control room ventilation TS Actions 
    to delete the Action statement to suspend all operations involving 
    positive reactivity changes, and adds an Applicability and Action 
    related to the movement of irradiated fuel assemblies. The changes also 
    add an Applicability footnote and revise the Bases to allow irradiated 
    fuel assemblies to be placed in a safe conservative position when 
    movement is required to be suspended. Other changes to the Bases are 
    being made to be consistent with the TS. These changes do not alter the 
    design or configuration of the plant. There has been no physical change 
    to plant systems, structures, or components. The proposed changes will 
    not reduce the ability of any of the safety-related equipment required 
    to mitigate Anticipated Operational Occurrences (AOOs) or accidents. 
    Therefore, the proposed changes will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this proposed 
    change involve a significant reduction in a margin of safety?
        Response: No.
        The proposed changes revise the control room TS Actions to delete 
    the Action statement to suspend all operations involving positive 
    reactivity changes, and adds an Applicability and Action related to the 
    movement of irradiated fuel assemblies. The changes also add an 
    Applicability footnote and revise the Bases to allow irradiated fuel 
    assemblies to be placed in a safe conservative position when movement 
    is required to be suspended. Other changes to the Bases are being made 
    to be consistent with the TS. The margin of safety is not affected 
    because the proposed changes to delete one Action and add an 
    Applicability and Action ensures the assumptions of the accident 
    analysis are being met. The administrative changes ensure the 
    applicable TS are entered and eliminate confusion associated with the 
    discrepancies between the TS and Bases. The more restrictive changes of 
    adding an Applicability and Action eliminates the precursor to an event 
    (fuel handling accident) that may release radioactivity when the 
    control room ventilation systems are inoperable. The less restrictive 
    changes revises the TS to rely on the instrumentation credited in the 
    accident analysis and to allow irradiated fuel assemblies to be placed 
    in a safe position to preclude a fuel handling accident. The 
    instruments are required to be operable per TS. Compliance with these 
    TS and also the SDM TS ensures that boron dilution event is precluded 
    or can be mitigated. Therefore, suspension of positive reactivity 
    changes is not required when the control room ventilation systems are 
    inoperable. These Actions ensure that appropriate measures are taken to 
    preclude events that would require the control room to be isolated when 
    any of the control room ventilation systems are inoperable. Therefore, 
    the proposed change will not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are
    
    [[Page 56249]]
    
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3 (Waterford 3), St. Charles Parish, Louisiana
    
        Date of amendment request: August 12, 1998
        Description of amendment request: The proposed amendment will 
    change Technical Specifications (TS) 3.1.2.8, 3.5.1, 3.5.4, Figure 3.1-
    1, and Bases 3/4.5.2 for Waterford 3. It increases the maximum boron 
    concentration in the Safety Injection Tanks (SITs) and the Refueling 
    Water Storage Pool (RWSP) from 2300 ppm to 2900 ppm.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this proposed 
    change involve a significant increase in the probability or consequence 
    of any accident previously evaluated?
        Response: No.
        The proposed change increases the maximum boron concentration in 
    the SITs and the RWSP from 2300 ppm to 2900 ppm. This change does not 
    affect the probability of any accident. This increase in boron 
    concentration affects the pH of water in the safety injection sump 
    during a LOCA [Loss of Coolant Accident] and the potential for boron 
    precipitation. The amount of TSP in containment is adequate to maintain 
    the pH above 7.0. The revised long term cooling analysis shows that 
    boron precipitation will not occur at the higher boron concentrations. 
    Therefore, this change will not adversely impact post-LOCA core 
    cooling. Thus, the consequences of a LOCA are not affected.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequence of any accident previously 
    evaluated.
        2. Will operation of the facility in accordance with this proposed 
    change create the possibility of a new or different kind of accident 
    from any accident previously evaluated?
        Response: No.
        The proposed change will not create any new system connection or 
    interactions. Thus, no new modes of failure are introduced. There is no 
    significant impact on the corrosion rate in the safety injection system 
    due to the slightly higher acidic solution with the higher boron 
    concentration.
        Therefore, the proposed change will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this proposed 
    change involve a significant reduction in margin of safety?
        Response: No.
        Sufficient TSP [Trisodium Phosphate Dodecahydrate] is provided in 
    the containment to ensure that the pH of the safety injection sump 
    water during a LOCA remains above 7.0 as stated in the Technical 
    Specification bases. Adequate time and HPSI [High Pressure Safety 
    Injection] flow exist to avoid boron precipitation during a LOCA. The 
    higher boron concentration limit will also allow higher refueling boron 
    concentrations which will increase the available shutdown margin.
        Therefore, the proposed change does not involve a significant 
    reduction in margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: John N. Hannon
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida
    
        Date of amendment request: August 31, 1998.
        Description of amendment request: The proposed amendment would 
    revise Improved Technical Specification (ITS) 5.6.2.10, ``Steam 
    Generator (OTSG [once-through steam generator]) Tube Surveillance 
    Program,'' to include a new repair process, called a ``repair roll'' or 
    ``re-roll.'' The process would be used to repair steam generator tubes 
    with defects within the upper tubesheet. Changes to inservice 
    inspection and reporting requirements are proposed for tubes which are 
    repaired using this process. The proposed revision would also require 
    inspection of both OTSGs during each inservice inspection. In addition, 
    several format and editorial changes are proposed to ITS 5.6.2.10 and 
    to ITS 5.7.2, ``Special Reports,'' for clarification purposes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed LAR [license amendment request] addresses several 
    editorial and format changes which do not impact accident analyses. LAR 
    #235 also proposes to implement the repair roll (re-roll) process.
        The qualification of the re-roll joint is based on establishing a 
    mechanical roll length which will carry all structural loads imposed on 
    the tubes with required margins. A series of tests and analyses were 
    performed to establish this length. Tests that were performed included 
    leak, tensile, fatigue, ultimate load and eddy current measurement 
    uncertainty. The analyses evaluated plant operating and faulted loads 
    in addition to tubesheet bow effects. Any tube leakage will be bounded 
    by the main steam line break (MSLB) evaluation presented in the Final 
    Safety Analysis Report (FSAR). The proposed change also requires 
    inspections of the joints created by the repair roll process. The 
    addition of this inspection does not change any accident initiators. 
    The proposed inspections after re-roll installation, and during future 
    inservice inspections, assure continuous monitoring of these tubes such 
    that inservice degradation of tubes repaired by the re-roll process 
    will be detected. Based on the Framatome Technologies qualification, as 
    well as the history for similar industry repair rolls, there are no new 
    safety issues, as defined in BAW-2303P, Revision 3, associated with the 
    repair roll. Therefore, this change does not involve a significant 
    increase in the probability or consequences of any accident previously 
    evaluated.
        (2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        No new failure modes or accident scenarios are created by the re-
    roll process. The new pressure boundary joint created by the repair 
    roll process
    
    [[Page 56250]]
    
    has been shown by testing and analysis to provide structural and 
    leakage integrity equivalent to the original design and construction 
    for all normal operating and accident conditions. Furthermore, the 
    testing and analysis demonstrate the repair roll process creates no new 
    adverse effects for the repaired tube and does not change the design or 
    operating characteristics of the OTSGs. In the unlikely event that a 
    tube with a repair roll should fail and sever completely at the 
    transition of the re-roll region, the tube would remain engaged in the 
    tubesheet bore, preventing interaction with other surrounding tubes. In 
    this case, leakage is bounded by the steam generator tube rupture 
    (SGTR) accident analysis. Therefore, this change does not create a 
    possibility of a new or different kind of accident from any previously 
    evaluated.
        (3) Involve a significant reduction in a margin of safety.
        The repair roll process effectively removes the defective/degraded 
    area of the tube from service. The new roll expanded interface created 
    with the tubesheet satisfies all the necessary structural, leakage and 
    heat transfer requirements. The joint is constrained within the 
    tubesheet bore; thus, there is no additional risk associated with tube 
    rupture. The accident leakage is shown to be well within the initial 
    assumption of the MSLB analysis of one gallon per minute primary-to-
    secondary leakage. Therefore, the FSAR analyzed accident scenarios 
    remain bounding, and the use of the repair roll process does not reduce 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
        Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC--A5A, P.O. Box 14042, St. Petersburg, Florida 
    33733-4042.
        NRC Project Director: Frederick J. Hebdon.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3 (CR-3), Citrus County, Florida
    
        Date of amendment request: August 31, 1998.
        Description of amendment request: The proposed amendment will 
    change the Improved Technical Specifications (ITS) to add three 
    additional Regulatory Guide (RG) 1.97 Type A Category 1 post-accident 
    monitoring (PAM) instrumentation variables and one Type B Category 1 
    PAM instrumentation variable to ITS Table 3.3.17-1, Post-Accident 
    Monitoring Instrumentation. The Type A Category 1 variables added are 
    low pressure injection (LPI) pump run status, LPI suction from reactor 
    building (RB) sump isolation valves DHV-42 and DHV-43 open position, 
    and high pressure injection (HPI) pump run status. The Type B Category 
    1 variable added is reactor coolant system (RCS) low range pressure.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        The addition of post-accident monitoring instrumentation to the CR-
    3 ITS and ITS Bases is to ensure instrumentation is available for use 
    by the operators for performing manual actions, or to verify automatic 
    actions have occurred, which are required to mitigate the effects of a 
    design basis accident. The instrumentation is used for monitoring by 
    the operators only after an accident occurs, performs no automatic 
    functions, and there are no credible failures of this instrumentation 
    which could initiate any accident previously evaluated. Therefore, the 
    probability of occurrence of any accident previously evaluated is 
    unaffected.
        The availability and use of this instrumentation ensures that the 
    prescribed manual operator actions for mitigating the consequences of 
    an accident will be implemented when necessary, and that the operator 
    has sufficient information to verify required automatic actions have 
    occurred when necessary. Therefore, the availability and use of the 
    instrumentation provides assurance that the consequences of accidents 
    will not be greater than that previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from previously evaluated accidents?
        The addition of post-accident monitoring instrumentation to the CR-
    3 ITS and ITS Bases is to ensure instrumentation is available for use 
    by the operators for performing manual actions, or to verify automatic 
    actions have occurred, which are required to mitigate the effects of a 
    design basis accident. The instrumentation is used for monitoring by 
    the operators only after an accident occurs, performs no automatic 
    functions, and there are no credible failures of this instrumentation 
    which could initiate a new or different kind of accident. Therefore, 
    the possibility of a new or different kind of accident occurring as a 
    result of this passive instrumentation is not created.
        3. Involve a significant reduction in a margin of safety?
        The addition of post-accident monitoring instrumentation to the CR-
    3 ITS and ITS Bases is to ensure instrumentation is available for use 
    by the operators for performing manual actions, or to verify automatic 
    actions have occurred, which are required to mitigate the effects of a 
    design basis accident. The instrumentation is used for monitoring by 
    the operators only after an accident occurs, and performs no automatic 
    functions. The availability and use of this instrumentation ensures 
    that the prescribed manual operator actions for mitigating the 
    consequences of an accident will be implemented when necessary, and 
    that the operator has sufficient information to verify required 
    automatic actions have occurred when necessary. These required manual 
    and automatic actions are necessary to preserve the margin of safety as 
    defined in the CR-3 ITS and ITS Bases. The availability and use of this 
    instrumentation provides assurance that the existing margin of safety 
    will be maintained, and assumptions related to the margin of safety 
    during mitigation of design basis accidents will be preserved. 
    Therefore, the existing margin of safety will not be reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
        Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC-A5A, P. O. Box 14042, St. Petersburg, Florida 
    33733-4042.
        NRC Project Director: Frederick J. Hebdon.
        GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey.
        Date of amendment request: May 5, 1998.
    
    [[Page 56251]]
    
        Description of amendment request: This request is to change the 
    licensing basis to allow for a small amount of containment overpressure 
    to ensure sufficient net positive suction head for the Emergency Core 
    Cooling System pumps under post Loss of Cooling Accident (LOCA) 
    conditions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change to the licensing basis does not ``Involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated * * * ''. As the strainers have no function until 
    after the design basis LOCA occurs, the design of the strainer cannot 
    affect the probability of a Large Break LOCA.
        The requested change to raise the assumed containment overpressure 
    for suction strainer design to 1.25 psig is less than that which is 
    already used in LOCA analyses for offsite releases. Therefore, this 
    change will not increase the offsite consequences of any previously 
    analyzed accident. The frequency of a design basis LOCA occurrence at 
    the Oyster Creek Nuclear Generating Station is conservatively estimated 
    at 5.67  x  10-4 per year. The frequency of a design basis 
    LOCA with a loss of containment overpressure is conservatively 
    estimated at 2.46  x  10-7 per year.
        Since the frequency of the design basis LOCA coincident with a loss 
    of containment overpressure is insignificant (2.46  x  
    10-7), the requested increase does not significantly impact 
    the probability of exceeding the existing design bases. The core damage 
    frequency increase due to the request for overpressure is mitigated, in 
    part, by the current procedural requirement to flood containment 
    following the design basis LOCA, thereby obviating the need for over 
    pressure in the long term. The risk evaluation, performed in support of 
    the request for over pressure, indicated a non-risk significant change 
    in the core damage frequency.
        The proposed change to the licensing bases does not ``Create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated * * *''. Both the new and existing strainers are 
    passive. They function solely to prevent debris from entering the 
    suction of the core and containment spray pumps. The only significant 
    difference is that the new strainers can remove more debris without 
    clogging. The slight amount of containment overpressure does not affect 
    the operation of the strainers, and improves the ability of the core 
    spray and containment spray systems to continue operation. Therefore, 
    no new or different kind of accident is created or possible.
        The proposed change to the licensing bases does not ``Involve a 
    significant reduction in a margin of safety * * *.'' The modification 
    increases the amount of debris that can be removed while maintaining 
    core spray system operation. The requested change takes credit for 1.25 
    psig of wetwell overpressure. However, as the requested change is 
    bounded by existing calculations for offsite release, no significant 
    reduction in the margin of safety can occur. Additionally, as 
    demonstrated in Attachment III, the probability of a LOCA with a loss 
    of containment overpressure is not significant.
        Guidance has been provided in ``Final Procedures and Standards on 
    No Significant Hazards Considerations,'' Final Rule, 51 FR 7744, for 
    the application of standards to license change requests for 
    determination of the existence of significant hazards considerations. 
    This document provided examples of amendments which are and are not 
    considered likely to involve significant hazards considerations.
        Based on the above evaluation and the review of 51 FR 7744, this 
    proposed change to the licensing basis of the Oyster Creek Nuclear 
    Generating Station does not involve irreversible changes, a significant 
    relaxation of the criteria used to establish safety limits, a 
    significant relaxation of the bases for the limiting safety system 
    settings, or a significant relaxation of the bases for the limiting 
    conditions for operations. Therefore, based on the guidance provided in 
    the Federal Register and the criteria established in 10 CFR 50.92(c), 
    the proposed change does not constitute a significant hazard.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
        Attorney for Licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cecil O. Thomas.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of amendment request: September 9, 1998.
        Description of amendment request: The proposed amendment would 
    change the Technical Specifications (TS) by: (1) Changing the TS 
    Definitions 1.24, ``Core Operating Limits Report,'' 1.27, ``Engineering 
    Safety Feature Response Time,'' and 1.31, ``Radiological Effluent 
    Monitoring and Offsite Dose Calculation Manual (REMODCM)''; (2) 
    changing TS 3.0.2, ``Limiting Condition For Operation,'' by adding a 
    new TS 3.0.6 to the Limiting Condition For Operation TS section; (3) 
    changing TS 4.0.5, ``Surveillance Requirements''; (4) changing the mode 
    applicability of TS 3.2.3, ``Total Unrodded Integrated Radial Peaking 
    Factor--FrT''; (5) changing TS 3.3.2.1, 
    ``Engineered Safety Features Actuation System Instrumentation,'' by 
    modifying TS Table 4.3-2 Table Notation (1) which it references; (6) 
    changing TS 3.4.1.1, ``Reactor Coolant System--Coolant Loops and 
    Coolant Circulation Startup and Power Operation'; and (7) changing TS 
    3.4.11, ``Reactor Coolant System--Reactor Coolant System Vents.'' The 
    associated TS Bases sections would also be updated to reflect the 
    proposed changes. The proposed changes would resolve identified 
    compliance issues.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
    Technical Specification Definitions
        The minor editorial and non-technical changes to correct reference, 
    spelling and terminology errors contained in the definitions will not 
    result in any technical changes to the Millstone Unit No. 2 Technical 
    Specifications. The proposed changes will have no adverse effect on 
    plant operation. Therefore, the proposed change will not result in a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
    Technical Specification 3.0.6
        The new Technical Specification, 3.0.6, will provide guidance on 
    returning inoperable equipment to service, under administrative 
    control, to demonstrate operability of that
    
    [[Page 56252]]
    
    equipment, or the operability or other equipment. Various Technical 
    Specification Actions require inoperable equipment to be removed from 
    service, such as maintaining a containment isolation valve closed or 
    tripping/bypassing a failed instrument channel. An exception to these 
    required actions is necessary to allow the performance of testing to 
    demonstrate the operability of the equipment being returned to service. 
    Specifically, this Technical Specification addresses the situation 
    where the inoperable equipment has been repaired, tested to the extent 
    possible, and believed to be capable of performing its function. At 
    this point, a presumption of the operability of the equipment is 
    reasonable, and is supported by experience. Therefore, it is acceptable 
    to place the equipment in service for testing under administrative 
    control. Administrative controls will be used to ensure the time the 
    equipment is returned to service is consistent with the Action 
    Statements and is limited to the time necessary to perform the 
    surveillance requirements.
        This specification will also allow the inoperable equipment to be 
    placed in a condition different from that required by the action 
    statement to demonstrate the operability of other equipment. An example 
    would be during the performance of an operability test on one reactor 
    protection channel while another channel associated with the same 
    function is inoperable. In this situation only one of the channels 
    could be in the tripped condition, otherwise a reactor trip would be 
    initiated. This is already permitted for reactor protection channels by 
    Technical Specifications 3.3.1.1, ``Instrumentation--Reactor Protective 
    Instrumentation,'' Action 2, and for engineered safety features 
    channels by 3.3.2.1, ``Instrumentation--Engineered Safety Feature 
    Actuation System Instrumentation,'' Action 2.
        This provision is provided only to perform surveillance 
    requirements to prove operability, and not to provide time to perform 
    any other preventive or corrective maintenance. The testing will be 
    performed consistent with the current Technical Specification Action 
    Statement and will be limited to the time necessary to perform the 
    surveillance requirement. The proposed changes will have no adverse 
    effect on plant operations. Therefore, the proposed change will not 
    result in a significant increase in the probability or consequences of 
    an accident previously evaluated.
    Technical Specification 4.0.5
        The proposed changes will revise Technical Specification 4.0.5.a 
    and Bases 3/4.4.10, ``Structural Integrity,'' by removing the phrase 
    ``(g), except where specific written relief has been granted by the 
    Commission pursuant to 10 CFR 50, Section 50.55a(g)(6)(i).'' The 
    changes to Technical Specifications clarify that all applicable 
    requirements in 10 CFR 50.55a apply. The changes relate to inservice 
    inspection (ISI) and inservice testing (IST) requirements which are 
    specified in 10 CFR 50.55a, ``Codes and Standards.'' The ISI and IST 
    requirements are given in 10 CFR 50.55a, which the licensee documents 
    via its 10 year interval program requirements. Upon finding a Code 
    requirement impractical because of limitations in the design (including 
    prohibitive dose rates), construction, or system configurations, NNECO 
    [Northeast Nuclear Energy Company] would be required to prepare the 
    determination describing the impractical condition(s) and the 
    applicable code requirements that cannot be met in accordance with 10 
    CFR 50.55a, paragraphs (f)(5)(iii) and (iv), and (g)(5)(iii) and (iv) 
    if within the first 12 months of a new interval. For example, 10 CFR 
    50.55a(f)(5)(iv), and (g)(5)(iv) allow a licensee up to a full year 
    after the beginning of an updated interval to inform the NRC of the new 
    Code requirements which cannot be met and to request relief. If an 
    impracticality is identified after the first 12 months, the guidance 
    contained in NUREG-1482 will be followed. This will eliminate 
    inconsistencies between the Technical Specifications and the 
    regulations. There will be no adverse effect on plant operations. 
    Therefore, the proposed changes will not result in a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
    Technical Specification 3.2.3
        The proposed change will change the mode of applicability for 
    Technical Specification 3.2.3 from Mode 1 to Mode 1 with thermal power 
    >20%. Data from the incore detectors are used for determining the 
    measured radial peaking factors to verify compliance with Technical 
    Specification 3.2.3. However, the accuracy of the neutron flux 
    information from the incore detectors is not reliable below 20% power. 
    The proposed change acknowledges this limitation of the incore 
    detectors by changing the applicability of this specification to power 
    levels where the data from the incore detectors is reliable. This will 
    have no adverse effect on plant operations since the current Technical 
    Specification surveillance requirements do not require the verification 
    of this limit until prior to operation above 70% following each fuel 
    loading, prior to 31 days accumulated operation in Mode 1, or if the 
    azimuthal power tilt limit is exceeded (Technical Specification 3.2.4 
    which is applicable in Mode 1 above 50% power). Therefore, the proposed 
    change has no impact on the initial conditions, with respect to power 
    distribution, assumed in the accident analysis. Thus, the proposed 
    change will not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
    Technical Specification 3.3.2.1
        The proposed change will add an exception to Technical 
    Specification 4.0.4 that will allow the channel functional test of the 
    automatic actuation logic associated with ESF [engineered safety 
    feature] actuations for safety injection, containment spray, 
    containment isolation, main steam line isolation, enclosure building 
    filtration, and containment sump recirculation to be delayed during 
    plant startup until the actuation blocks are removed. This will allow 
    entry into Mode 3 where plant conditions (sufficient pressurizer and 
    steam generator pressure) can be established that will automatically 
    remove the blocks of these ESF actuations. The channel functional test 
    of the automatic actuation logic, using the ATI [Automatic Testing 
    Insertor] circuit, will then be performed. In addition, the channel 
    functional tests of the automatic actuation logic must be performed 
    prior to entering Mode 2.
        The exception to Technical Specification 4.0.4 allows a mode change 
    with equipment that is inoperable only because conditions [cannot] be 
    established to perform the SR [surveillance requirement] until after 
    the mode is entered. All other equipment operability requirements must 
    be met. Even though operability of the automatic actuation logic for 
    the affected ESF actuations cannot be verified prior to entering Mode 
    3, this equipment is still expected to be operable. The ESFAS 
    [engineered safety feature actuation system] will continue to function 
    as before. Therefore, the proposed change will not result in a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
    Technical Specification 3.4.1.1
        The Flow Dependent Setpoint Selector Switch was installed to allow 
    power operation with less than four reactor coolant pumps (RCPs) in 
    operation by changing the reactor trip setpoints for the variable high 
    power, Reactor Coolant System (RCS) low flow,
    
    [[Page 56253]]
    
    and thermal margin low pressure (TM/LP) reactor trips. Millstone Unit 
    No. 2 is not currently licensed to operate with less than four RCPs in 
    operation. Therefore, this switch should be maintained in the four pump 
    position.
        The use of the switch position to ensure compliance with Technical 
    Specification 3.4.1.1 provides an indirect verification of LCO 
    [limiting condition for operation] compliance since the loss of an RCP 
    will result in a reactor trip when in the four pump position. The 
    proposed change will replace the method used for LCO verification with 
    one that is more consistent with the LCO. Verification of switch 
    position is performed as a prerequisite prior to reactor startup 
    (entering Mode 2). It is not necessary to verify the switch position 
    every 12 hours as currently required. The position of this switch is 
    important to the operability of the associated Reactor Protection 
    System (RPS) trips variable high power, RCS low flow, and TM/LP). The 
    operability of these RPS trips and associated setpoints is already 
    covered by Technical Specifications 2.2.1, ``Reactor Trip Setpoints,'' 
    and 3.3.1.1, ``Reactor Protective Instrumentation.''
        It is not necessary to verify the position of this switch fifteen 
    minutes prior to reactor criticality since the switch position is 
    verified prior to a reactor startup, and is not expected to be changed 
    during power operation. If surveillance testing or maintenance 
    activities are to be performed which may require the switch to be in 
    other than the four pump position, the affected RPS channels will 
    already have been removed from service (declared inoperable and placed 
    in the tripped or bypassed condition) prior to commencing the 
    activities. In addition, a light (``PUMP SETPOINT ERROR'') on each of 
    the RPS Calibration and Indication Panels will illuminate if the switch 
    is not in the four pump position.
        It is also not necessary to verify compliance with the requirements 
    of Technical Specification 3.4.1.1 within fifteen minutes prior to 
    reactor criticality since this condition is verified prior to a reactor 
    startup, and the RPS will initiate a reactor trip if less than four 
    RCPs are in operation.
        The proposed change will replace SR 4.4.1.1, verification of the 
    Flow Dependent Setpoint Selector Switch position, with a verification 
    check of the required RCS loops. This verification is more consistent 
    with the Limiting Condition for Operation (LCO). This will not change 
    the requirement that both RCS loops be operable and operating in Modes 
    1 and 2. The Technical Specification will continue to assure that the 
    initial condition, with respect to RCS loops in service, in the 
    accident analysis is applicable. Therefore, the proposed change will 
    not result in a significant increase in the probability or consequences 
    of an accident previously evaluated.
    Technical Specification 3.4.11
        The proposed change to modify the wording of SR 4.4.11.3 will not 
    affect the operability requirements of the RCS Vent System. This change 
    will provide operational flexibility to use a series of overlapping 
    tests to verify flow through sections of the vent system, such that 
    when completed, flow will be verified through all parts of the vent 
    system. This will minimize potential contamination of the area 
    surrounding the sparger and will eliminate the need to establish solid 
    water conditions in the RCS.
        The proposed surveillance requirement will still verify the ability 
    of the vent valves to operate. This will provide reasonable assurance 
    of system operability and availability if needed to mitigate the 
    consequences of design basis accidents. Therefore, the proposed change 
    will not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes have no adverse effect on any of the design 
    basis accidents previously evaluated or on any equipment important to 
    safety. Therefore, the license amendment request does not impact the 
    probability of an accident previously evaluate nor does it involve a 
    significant increase in the consequences of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes will not alter the plant configuration (no new 
    or different type of equipment will be installed) or require any new or 
    unusual operator actions. They do not alter the way any structure, 
    system, or component functions and do not alter the manner in which the 
    plant is operated. The proposed changes do not introduce any new 
    failure modes. Therefore, the proposed changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes will correct reference, spelling, and 
    terminology errors in various Technical Specification Definitions; add 
    a new Technical Specification, 3.0.6; modify Technical Specification 
    4.0.5 to remove an inconsistency between the Technical Specification 
    and the regulations; change the applicability of Technical 
    Specification 3.2.3; add an exception to Technical Specification 4.0.4 
    to Technical Specification 3.3.2.1; modify the wording of a 
    surveillance requirement associated with RCS Technical Specification 
    3.4.1.1; and modify the wording of a surveillance requirement 
    associated with the RCS Vent System, Technical Specification 3.4.11 to 
    provide operational flexibility in the performance of the test. These 
    changes will have no adverse effect on equipment important to safety. 
    The equipment will continue to function as assumed in the design basis 
    accident analysis. Therefore, there will be no significant reduction of 
    the margin of safety as defined in the Bases for the Technical 
    Specifications affected by these proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    Connecticut.
        NRC Project Director: William M. Dean.
    
    Philadelphia Electric Company, Docket No. 50-353, Limerick Generating 
    Station, Unit 2, Montgomery County, Pennsylvania
    
        Date of amendment request: September 14, 1998.
        Description of amendment request: The proposed amendment to the 
    Limerick Generating Station (LGS), Unit 2, Technical Specifications 
    (TS) would revise TS Table 4.4.6.1.3-1, ``Reactor Vessel Material 
    Surveillance Program--Withdrawal Schedule.'' This table provides the 
    schedule for withdrawing the reactor pressure vessel material 
    surveillance program capsules. This proposed TS change involves 
    revising the schedule for withdrawing the first surveillance capsule 
    from 8 Effective Full Power years (EFPY) to 15 EFPY, and the second 
    surveillance capsule from 20 EFPY to 30 EFPY.
    
    [[Page 56254]]
    
        A revision to TS Surveillance Requirement (SR) 4.4.6.1.4 is also 
    proposed. This revision will remove the reference to flux wire removal 
    and analysis that was originally required following the first cycle of 
    operation. TS SR 4.4.6.1.4 will be changed to refer to the flux wires 
    that are located within the surveillance capsules, which will be 
    removed and analyzed in accordance with the surveillance capsule 
    removal schedule, located in Table 4.4.6.1.3-1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed changes do not increase the probability of occurrence 
    of an accident previously evaluated in the safety analysis report and 
    do not affect any accident initiators as described in the Safety 
    Analysis Report (SAR). The change revises the withdrawal schedule for 
    the reactor vessel material surveillance capsules. The capsules are not 
    an initiator of any previously analyzed accident nor does the 
    withdrawal schedule of the surveillance capsules affect the probability 
    or consequences of any previously analyzed accident.
        The proposed changes will not affect the Pressure-Temperature (P-T) 
    limits as specified in LGS TS Figure 3.4.6.1-1 and Updated Final Safety 
    Analysis Report (UFSAR) Figure 5.3-4. P-T limits are imposed on the 
    reactor coolant system to ensure that adequate safety margins exist 
    during normal operation, anticipated operational occurrences, and 
    system hydrostatic tests. The P-T limits are related to the 
    RTNDT [reference temperatures], as described in ASME Section 
    III, Appendix G. Changes in the fracture toughness properties of RPV 
    [reactor pressure vessel] beltline materials, resulting from neutron 
    irradiation and the thermal environment, are monitored by a 
    surveillance program in compliance with the requirements of 10 CFR 50 
    Appendix H. The effect of neutron fluence on the shift in the 
    RTNDT is predicted by methods given in Regulatory Guide 
    1.99, Rev.2.
        As detailed in Attachment 3 [of the September 14, 1998, submittal], 
    for LGS, Unit 2, the combination of low expected RTNDT shift 
    for the plate material due to low predicted fluence and excellent 
    material chemistry; Supplemental Surveillance Program (SSP) data on 
    similar material; and the inherent margin in the P-T curve 
    calculations, with the withdrawal schedule of the first surveillance 
    capsule modified from 8 EFPY to 15 EFPY and the second surveillance 
    capsule modified from 20 EFPY to 30 EFPY, will result in more credible 
    sets of surveillance data, while ensuring the continued safe operation 
    of LGS, Unit 2.
        The current LGS P-T limits were established based on adjusted 
    reference temperatures developed in accordance with the procedures 
    prescribed in Regulatory Guide 1.99, Revision 2, Regulatory Position 1, 
    ``Surveillance Data Not Available.'' Calculation of adjusted reference 
    temperature by these procedures includes a conservative base fluence 
    estimate; power rerate adjustment of a 110% fluence multiplier from 
    startup, instead of a 105% fluence multiplier since 2R03 [third 
    refueling outage]; and a margin term to ensure conservative, upper-
    bound values are used for the calculation of the P-T limits. Revision 
    of the first capsule withdrawal schedule will not affect the P-T limits 
    because they will continue to be established in accordance with 
    Regulatory Position 1 guidance. Also, as indicated in Attachment 3, it 
    is also appropriate to extend the withdrawal of the LGS, Unit 2, second 
    capsule. The current schedule specifies withdrawal of the second 
    capsule at 20 EFPY. Based upon the information provided in Attachment 3 
    supporting withdrawal of the first capsule at 15 EFPY, there will be an 
    insignificant shift in material properties at 20 EFPY, after only an 
    additional exposure of 5 EFPY. It is appropriate to extend this 
    schedule to 30 EFPY which meets the intent of ASTM E185-82, such that 
    the withdrawal of the second capsule occurs before the accumulated 
    neutron fluence of the capsule corresponds to the approximate EOL [end 
    of life] fluence at the reactor pressure vessel inner wall location, 
    and provides consistency with the LGS, Unit 1, withdrawal schedule.
        In accordance with the guidance stipulated in Regulatory Guide 
    1.99, ``Radiation Embrittlement of Reactor Vessel Materials,'' Revision 
    2, Regulatory Position 2, ``Surveillance Data Available,'' the 
    collection of two (2) or more sets of credible surveillance data is 
    necessary to empirically calculate the adjusted reference temperature 
    (ART). Each surveillance capsule constitutes one set of credible 
    surveillance data. This calculated ART can be used to revise the P-T 
    curves (TS Figure 3.4.6.1-1). Without two (2) or more sets of credible 
    data, the ART must be calculated and the P-T curves revised, based upon 
    the calculational methodologies as provided in the Regulatory Guide 
    1.99, Revision 2, Regulatory Position 1, ``Surveillance Data Not 
    Available.'' These methodologies use plant specific chemistry and 
    fluence values to determine a calculated shift in RTNDT. A 
    ``margin'' term is then added, to obtain conservative, upper-bound 
    values of adjusted reference temperature.
        The existing LGS, Unit 2, P-T curves are based upon the Regulatory 
    Position 1 methodology, and are currently valid up to 10 EFPY. With 
    first capsule removal at either 8 or 15 EFPY, the existing P-T curves 
    will require a revision, prior to reaching 10 EFPY, based upon the 
    calculational methodologies as contained in the Regulatory Guide 1.99, 
    Revision 2, Regulatory Position 1, ``Surveillance Data Not Available.'' 
    Therefore, the Technical Specification revision to the first capsule 
    withdrawal schedule, as supported by this Safety Evaluation [supporting 
    information described in attachments 1 and 3 of the September 14, 1998, 
    submittal], results in no impact to the calculational methodologies 
    that will be used for the P-T curve revision that will be necessary to 
    extend the curves beyond 10 EFPY.
        The fluence data as determined from the surveillance capsule flux 
    wires at 15 EFPY will provide an accurate indication of neutron 
    fluence. In accordance with Regulatory Guide 1.99, Revision 2, 
    Regulatory Position 1 methodology, data from these flux wires will 
    permit an adjustment of TS Figure 3.4.6.1-1 in accordance with TS SR 
    4.4.6.1.3, if required, and will meet the requirements of 10 CFR 50, 
    Appendix H, and ASTM E-185.
        The proposed changes will not affect any plant safety limits or 
    limiting conditions of operation. The proposed changes will not affect 
    reactor pressure vessel performance as it involves no physical changes 
    and LGS P-T limits will remain conservative in accordance with 
    Regulatory Guide 1.99, Revision 2, guidance. The proposed changes will 
    not cause the reactor pressure vessel or interfacing systems to be 
    operated outside of their design or testing limits.
        The proposed changes do not increase the probability of the 
    occurrence of a malfunction, or consequences of a malfunction, of 
    equipment important to safety previously evaluated in the SAR. The 
    proposed changes do not involve any physical changes to equipment 
    important to safety. The potential for reactor vessel failure will be 
    adequately assessed by the proposed withdrawal schedule. In addition, 
    the results from
    
    [[Page 56255]]
    
    the Supplemental Surveillance Program (SSP) will provide industry data 
    that bounds the materials used in the LGS vessel until the data from 
    the first LGS capsule is available. The proposed change provides the 
    same level of confidence in the integrity of the vessel. The P-T curves 
    are currently controlled by the TS and are determined using the 
    conservative methodology delineated in Regulatory Guide 1.99. 
    Therefore, the possibility of failure of the reactor vessel is not 
    increased. The current P-T limit curves are inherently conservative and 
    will continue to be adhered to.
        Therefore, the proposed TS changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed changes do not create the possibility of a different 
    type of accident than any previously evaluated in the SAR. The proposed 
    changes are a revision of the withdrawal schedule for the first reactor 
    pressure vessel material surveillance capsule from 8 EFPY to 15 EFPY, 
    and for the second capsule from 20 EFPY to 30 EFPY. The proposed 
    changes do not involve a physical modification of the design of plant 
    structures, systems, or components. The proposed changes will not 
    impact the manner in which the plant is operated as plant operating and 
    testing procedures will not be affected by the change. No new accident 
    types or failure modes will be introduced as a result of the proposed 
    change.
        LGS's current P-T limits were established based on adjusted 
    reference temperatures developed in accordance with the procedures 
    prescribed in Regulatory Guide 1.99, Revision 2, Regulatory Position 1, 
    ``Surveillance Data Not Available.'' Calculation of adjusted reference 
    temperature by these procedures includes a conservative base fluence 
    estimate; power rerate adjustment of a 110% fluence multiplier from 
    startup, instead of a 105% fluence multiplier since 2R03; and a margin 
    term to ensure conservative, upper-bound values are used for the 
    calculation of the P-T limits. Revision of the first capsule withdrawal 
    schedule will not affect the P-T limits because they will continue to 
    be established in accordance with the guidance of Regulatory Position 1 
    of Regulatory Guide 1.99. Also, as specified in Attachment 3, it is 
    appropriate to extend the withdrawal of the LGS, Unit 2, second 
    capsule. The current schedule specifies withdrawal of the second 
    capsule at 20 EFPY. Based upon the information provided in Attachment 3 
    supporting withdrawal of the first capsule at 15 EFPY, there will be an 
    insignificant shift in material properties at 20 EFPY, after only an 
    additional exposure of 5 EFPY. It is appropriate to extend this 
    schedule to 30 EFPY which meets the intent of ASTM E185-82, such that 
    the withdrawal of the second capsule occurs before the accumulated 
    neutron fluence of the capsule corresponds to the approximate EOL 
    fluence at the reactor inner wall location, and provides consistency 
    with the LGS, Unit 1, withdrawal schedule.
        The existing LGS, Unit 2, P-T curves are based upon the Regulatory 
    Position 1 methodology, and are currently valid up to 10 EFPY. With 
    first capsule removal at either 8 or 15 EFPY, the existing P-T curves 
    will require a revision, prior to reaching 10 EFPY, based upon the 
    calculational methodologies as contained in the Regulatory Guide 1.99, 
    Revision 2, Regulatory Position 1, ``Surveillance Data Not Available.'' 
    Therefore, the proposed TS revision to the first capsule withdrawal 
    schedule results in no impact to the calculational methodologies that 
    will be used for the P-T curve revision that will be necessary to 
    extend the curves beyond 10 EFPY.
        The fluence data as determined from the surveillance capsule flux 
    wires at 15 EFPY will provide an accurate indication of neutron 
    fluence. In accordance with Regulatory Guide 1.99, Revision 2, 
    Regulatory Position 1 methodology, data from these flux wires will 
    permit an adjustment of TS Figure 3.4.6.1-1 in accordance with TS SR 
    4.4.6.1.3, if required, and will meet the requirements of 10 CFR 50, 
    Appendix H, and ASTM E-185.
        The potential for reactor vessel failure will be adequately 
    assessed by the proposed withdrawal schedule. In addition, the results 
    from the SSP will provide industry data that bounds the materials used 
    in the LGS vessel, until the data from the first LGS capsule is 
    available. The proposed changes provide the same level of confidence in 
    the integrity of the vessel . The P-T curves are currently controlled 
    by the TS and are determined using the conservative methodology in 
    Regulatory Guide 1.99. Therefore, the possibility of failure of the 
    reactor vessel is not increased. The current P-T limit curves are 
    inherently conservative and will continue to be adhered to.
        Therefore, the proposed TS changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed TS changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes to the TS do not reduce the margin of safety 
    as defined in the Bases for any TS. The proposed changes will not 
    affect any safety limits, limiting safety system settings, or limiting 
    conditions of operation. The proposed changes do not represent a change 
    in initial conditions, system response time, or in any other parameter 
    affecting the course of an accident analysis supporting the Bases of 
    any TS. The proposed changes do not involve revision of the P-T limits, 
    but rather a revision of the withdrawal schedule for the surveillance 
    capsules. The current P-T limits were established based on the adjusted 
    reference temperatures for reactor pressure vessel beltline materials 
    calculated in accordance with the guidance stipulated in Regulatory 
    Position 1 of Regulatory Guide 1.99, Revision 2. P-T limits will 
    continue to be revised as necessary for changes in adjusted reference 
    temperature due to changes in fluence according to Regulatory Position 
    1 until two (2) or more credible surveillance data sets becomes 
    available. When two (2) or more credible surveillance data sets become 
    available, P-T limits will be revised as prescribed by Regulatory 
    Position 2 of Regulatory Guide 1.99, Revision 2, or other NRC approved 
    guidance.
        The current P-T limit curves are inherently conservative and 
    provide sufficient margin to ensure the integrity of the reactor 
    vessel. The changes do not adversely affect these curves. The fluence 
    data as determined from the surveillance capsule flux wires at 15 EFPY 
    will provide an accurate indication of neutron fluence. In accordance 
    with Regulatory Guide 1.99, Revision 2, Regulatory Position 1 
    methodology, data from these flux wires will permit an adjustment of TS 
    Figure 3.4.6.1-1 in accordance with TS SR 4.4.6.1.3, if required, and 
    will meet the requirements of 10 CFR 50, Appendix H, and ASTM E-185.
        Therefore, the proposed TS changes do not involve a reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
    
    [[Page 56256]]
    
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, PA 19101.
        NRC Project Director: Robert A. Capra.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: April 16, 1998.
        Description of amendment request: This application for amendment to 
    the Indian Point 3 Technical Specifications (TSs) proposes to modify a 
    testing requirement for the emergency diesel generators (EDGs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident previously 
    analyzed?
        Response:
        No. The three Emergency Diesel Generators (EDG) at Indian Point 3 
    are designed to provide a source of power to support a safe and orderly 
    plant shutdown in the event that all other normal and standby sources 
    of power are not available, such as during a postulated Loss of Offsite 
    Power (LOOP). The probability of such events occurring is not affected 
    by the proposed amendment. Any two of the three EDGs are capable of 
    supplying the minimum power requirements for emergency safeguards 
    equipment that mitigate the consequences of postulated design basis 
    accident conditions. Periodic preventive maintenance and surveillance 
    testing are performed to provide assurance that the operability of all 
    three EDGs is maintained. In the event that an inoperable EDG is 
    identified, both the existing specification and the proposed change 
    provide for actions that verify the operability of the remaining 2 
    EDGs. Operability of 2 EDGs ensures that sufficient emergency power is 
    available, if needed, to mitigate the consequences of postulated 
    accidents. Therefore, the proposed license amendment does not involve a 
    significant increase in the probability or consequences of an accident 
    previously analyzed.
        (2) Does the proposed license amendment create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated?
        Response:
        No. The proposed license amendment does not involve any physical 
    changes to plant systems or component setpoints. Also, there are no 
    changes to the way in which systems or equipment are operated. The 
    proposed change will continue to require that the operability of the 
    remaining two EDGs be verified if one of the three EDGs is found to be 
    inoperable. The proposed change to allow the use of a common cause 
    failure evaluation, as an alternative to testing, to accomplish the 
    operability verification can benefit overall EDG reliability by 
    eliminating unnecessary EDG starts. Therefore, the proposed license 
    amendment does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Does the proposed amendment involve a significant reduction in 
    a margin of safety?
        Response:
        No. Important performance requirements for the EDGs include 
    electrical output capacity, elapsed time to start and reach rated 
    output, and fuel storage supply to support a minimum period of 
    operation. The proposed amendment does not change EDG performance 
    requirements. The existing specification allows a period of 24 hours in 
    which to verify the operability of the remaining 2 EDGs if one of the 
    three EDGs is found inoperable. The proposed amendment does not change 
    the 24-hour time limit. Operability verification, either by testing or 
    evaluation, within 24 hours provides assurance that this source of 
    emergency power is available if needed. Therefore, the proposed 
    amendment does not involve a significant reduction in a margin of 
    safety. Also, this verification method has been approved for use with 
    the current Standard Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. David E. Blabey, 10 Columbus Circle, New 
    York, New York 10019.
        NRC Project Director: S. Singh Bajwa, Director
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: April 16, 1998, as supplemented August 
    20, 1998.
        Description of amendment request: This application for amendment to 
    Table 4.1-1 of the Indian Point 3 Technical Specifications (TSs) 
    proposes to change surveillance frequency requirements for the various 
    instrument channels to accommodate a 24-month operating cycle. The 
    proposed amendment also revises Section 6 of the TSs to reflect updated 
    analyses.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Does the proposed license amendment involve a significant increase 
    in the probability or consequences of an accident previously analyzed?
        Response:
        No. The proposed license amendment to extend the calibration 
    surveillance frequency of the following instrument channels is being 
    made to support plant operation with a 24-month fuel cycle:
        (a) Pressurizer Water Level
        (b) Accumulator Level and Pressure
        (c) Reactor Coolant System Subcooling Margin Monitor
        (d) Core Exit Thermocouples
        (e) Reactor Vessel Level Indication System
        Changing the calibration intervals for these instrument channels 
    neither directly nor indirectly affects the initiation or probability 
    of any previously analyzed accident. The changes do not affect the 
    integrity of any of the principal barriers against radiation release 
    (fuel cladding, reactor vessel, and containment building). The ability 
    of the plant to mitigate the consequences of any previously analyzed 
    accidents is not adversely affected. Evaluation of the proposed change 
    to the surveillance interval demonstrates that licensing basis safety 
    analyses acceptance criteria and Indian Point 3 Emergency Operating 
    Procedure (EOP) criteria continue to be met.
        Item (a) provides an input to the Reactor Protection System (RPS) 
    to initiate a reactor trip if the measured parameters exceed specified 
    values. Item (b) is used by control room operators to ensure that the 
    accident mitigation capability of the accumulators is maintained within 
    specified limits. Items (c), (d), and (e)
    
    [[Page 56257]]
    
    provide post-accident information to control room operators to support 
    recovery efforts. Item (d) is also used to monitor core performance for 
    fuel management activities.
        The proposed new surveillance frequency for these instrument 
    channels was evaluated using the guidance of Generic Letter 91-04. The 
    basis for the changes includes a quantitative evaluation of instrument 
    drift. Also, loop accuracy/setpoint calculations were updated to 
    accommodate the extended surveillance period. Analyses and evaluations 
    completed to assess the proposed increase in the surveillance interval 
    demonstrate that the effectiveness of these instruments in fulfilling 
    their respective functions is maintained. Channel checks required to be 
    performed each shift or each day, according to Technical Specifications 
    for the subject channels, will continue to be performed to provide 
    assurance of instrument channel operability. Therefore, the proposed 
    amendment does not involve a significant increase in the probability or 
    consequences of any previously analyzed accident.
        Does the proposed license amendment create the possibility of a new 
    or different kind of accident from any accident previously evaluated?
        Response:
        No. The increased calibration surveillance intervals for the above 
    listed instrument channels were justified based on evaluation of past 
    equipment performance and do not require any plant hardware changes or 
    changes in normal system operation. Changing the calibration intervals 
    for these channels neither directly nor indirectly has any means of 
    creating the possibility of a new or different kind of accident. 
    Certain alarm and EOP setpoint changes will be made consistent with the 
    revised uncertainty calculations for the subject channels. These new 
    setpoints and related operator responses support existing accident 
    mitigation strategies and do not create the possibility of a new or 
    different kind of accident from any previously analyzed. Therefore, 
    there are no new failure modes introduced as a result of extending 
    these surveillance intervals, and the proposed amendment does not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        Does the proposed amendment involve a significant reduction in a 
    margin of safety?
        Response:
        No. Pressurizer water level instrumentation provides input to the 
    reactor protection system and to the pressurizer water level control 
    system. Pressurizer water level, as indicated by the selected control 
    channel, is used to establish the initial condition pressurizer water 
    level assumption for certain UFSAR [Updated Final Safety Analysis 
    Report] Chapter 14 safety analyses. The proposed change to the 
    calibration surveillance interval was evaluated using the criteria of 
    95% probability/95% confidence level for process sensor drift. The loop 
    accuracy/setpoint calculations were updated for the level channels to 
    demonstrate the acceptability of the proposed increase in the 
    surveillance interval. There are no changes required to the limiting 
    safety system setting (LSSS) stated in the Technical Specifications for 
    these channels. The LSSS for high pressurizer water level will remain 
    at [less than or equal to] 92% of span. The margin of safety between 
    the specified LSSS value required by Technical Specifications and the 
    safety limit used in the UFSAR Chapter 14 safety analyses is unchanged.
        The instrument channels for accumulator pressure and level do not 
    provide input to the reactor protection system or the engineered safety 
    features system. These instruments provide alarms and indication to 
    control room operators to maintain accumulator cover gas pressure and 
    water volume within specified limits. They are also used for 
    establishing initial condition accumulator pressure and level 
    assumptions for certain UFSAR Chapter 14 safety analyses. Accordingly, 
    the process sensor drift analysis was performed using the criteria of 
    95% probability/75% confidence level.
        The remaining three instrument channels addressed by this proposed 
    license change are used to provide indication of adequate core cooling 
    following certain hypothetical accident conditions. These instrument 
    channels are not associated with any margin of safety specified by the 
    Technical Specifications, and they are not factors in any UFSAR Chapter 
    14 safety analyses. However, they are factored into the calculations of 
    pertinent setpoints used in alarm response procedures and EOPs. The 
    updated drift and uncertainty calculations and evaluations for these 
    instrument channels demonstrate that applicable accuracy requirements 
    for Indian Point 3 are satisfied with the proposed new surveillance 
    intervals. The instrument channels will remain effective to support 
    plant operator implementation of the Emergency Operating Procedures, 
    which are consistent with the Westinghouse Owners' Group Emergency 
    Response Guidelines.
        Changing the calibration interval for these channels does not 
    affect margin of safety for previously analyzed accidents. Also, the 
    evaluation of related changes to UFSAR Chapter 14 safety analyses input 
    assumptions has demonstrated that licensing basis safety analysis 
    acceptance criteria and EOP criteria continue to be met, and previously 
    existing margins based on these pertinent acceptance criteria continue 
    to be maintained.
        Therefore, the proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. The staff has also reviewed the licensee's proposed change 
    to reflect updated safety analyses in Section 6 of the TSs and it 
    appears that the three standards of 50.92(c) are satisfied for these 
    changes as well. Therefore, the NRC staff proposes to determine that 
    the amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. David E. Blabey, 10 Columbus Circle, New 
    York, New York 10019.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment request: September 17, 1998.
        Description of amendment request: The amendments would revise 
    Technical Specification (TS) 3/4.8.2, ``Electrical Power Sources--
    Shutdown,'' for the AC distribution system and the 125-volt and 28-volt 
    DC distribution systems. Specifically, the amendments would change the 
    Applicability and Action Statements, if less than the complement of 
    equipment and busses are operable, to eliminate the need to establish 
    containment integrity and to add the action to suspend core 
    alterations, positive reactivity additions, and movement of irradiated 
    fuel assemblies.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will not involve a significant increase in the probability or
    
    [[Page 56258]]
    
    consequences of an accident previously evaluated.
        In Modes 1 through 4 [power operation through hot shutdown], a 
    Design Basis Accident would cause the release of radioactive material 
    into the containment. Release of that radioactive material to the 
    environment is prevented during operation in Modes 1 through 4 by 
    maintaining containment integrity. In Modes 5 and 6 [cold shutdown and 
    refueling] the probability and consequences of this event are lower 
    because of the reduced reactor coolant pressure and temperature 
    limitations of these modes.
        A minimum complement of electrical power sources and distribution 
    systems is established in Modes 5 and 6 to assure that adequate 
    electrical power is available to mitigate the consequences of a fuel 
    handling accident. Because of the lack of containment pressurization 
    potential during a fuel handling accident, less stringent requirements 
    are needed to isolate containment from the outside atmosphere. These 
    requirements are applied during refueling operations by Technical 
    Specification 3.9.4, Refueling Operations, Containment Building 
    Penetrations. Technical Specification 3.9.4 is applicable in Mode 6 and 
    establishes containment closure vice containment integrity during 
    refueling operation (core alterations and movement of irradiated fuel 
    within containment).
        In Mode 5, fuel handling is generally limited to placement of new 
    fuel prior to core off load or movement of irradiated fuel within the 
    spent fuel pool. Because the Spent Fuel Pool is not located within 
    containment, establishment of either containment integrity or 
    containment closure would not help to mitigate the consequences of a 
    fuel handling accident in that area. Mitigation of a fuel handling 
    accident is accomplished through Technical Specification 3.9.12, 
    Refueling Operations, Fuel Handling Area Ventilation System, which 
    requires that the Fuel Handling Area Ventilation system be operable 
    whenever irradiated fuel is present in the storage pool. This insures 
    that all radioactive material released from the rupture of an 
    irradiated fuel assembly would be filtered through filtration equipment 
    prior to discharge to the atmosphere.
        With the number of energized A.C. or D.C. power distribution 
    systems less than the required, sufficient power may not be available 
    to recover from a fuel handling accident. Consequently, the Action 
    statements require immediate suspension of all operations involving 
    core alterations, positive reactivity changes, and movement of 
    irradiated fuel assemblies. This precludes the possibility of a fuel 
    handling accident and the need for containment integrity.
        Based upon the above, the proposed change will not increase the 
    probability or consequences of an accident previously analyzed.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed changes do not require any change in the configuration 
    or operation of the plant. Specifically, no new hardware is being added 
    to the plant as part of the proposed change, no existing equipment is 
    being modified, and no significant changes in operations are being 
    introduced. Therefore, these changes will not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Will not involve a significant reduction in a margin of safety.
        The proposed change will not alter any assumptions, initial 
    conditions, or results of any accident analyses. The proposed 
    additional Applicability will ensure proper operation of the Fuel 
    Handling Area Ventilation system during movement of irradiated fuel in 
    the spent fuel pool. The proposed ACTIONS, to be taken in the event 
    that the LCO [limiting condition for operation] is not met, will 
    preclude the conditions that would lead to the need for establishing 
    containment integrity. The change will, therefore, not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Project Director: Robert A. Capra.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment request: September 29, 1998.
        Description of amendment request: The proposed amendments would 
    revise Technical Specification 3/4.9.4, ``Refueling Operations, 
    Containment Building Penetrations,'' to permit the use of equivalent 
    methods to obtain containment closure during refueling operations. 
    Specifically, the proposed changes would allow the installation of an 
    outage equipment door or other closure devices that are capable of 
    providing access for temporary services needed to support maintenance 
    activities within containment.
        In addition to the above changes, the terminology for the 
    Containment Equipment Hatch inside door used in LCO 3.9.4.a is being 
    changed. The term ``Containment Equipment Door'' is being changed to 
    ``Containment Equipment Hatch Inside Door'' to bring it into agreement 
    with the terminology used in Salem design documents.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        In Modes 1 through 4 [power operations through hot shutdown], a 
    Design Basis Accident would cause the release of radioactive material 
    into the containment. The release of radioactive material from the 
    containment to the environment is prevented during operation in Modes 1 
    through 4 by maintaining CONTAINMENT INTEGRITY. In Mode 5 and 6 [cold 
    shutdown and refueling] the requirements to prevent releases from the 
    containment to the environment from postulated accidents are less 
    stringent because of the reduced reactor coolant pressure and 
    temperature limitations of these modes. In all cases, the containment 
    serves as a passive barrier to mitigate the consequences of accidents 
    analyzed. The containment is not considered to be a contributor to the 
    probability of those accidents. Therefore, this change, which will 
    permit the use of equivalent methods for establishing containment 
    closure during refueling operations, will not increase the probability 
    of an accident previously analyzed.
        During refueling operations, a release of radioactive material to 
    the containment could occur as the result of a fuel handling accident. 
    Actions are taken to mitigate the consequences of a fuel handling 
    accident inside containment during refueling operations through 
    application of technical specification requirements for Refueling 
    Cavity water level, minimum decay time prior to CORE ALTERATIONS, and 
    Containment Building Penetrations.
        Because of the lack of containment pressurization potential and the 
    reduced
    
    [[Page 56259]]
    
    source term during a fuel handling accident, less stringent 
    requirements are needed to isolate containment from the outside 
    atmosphere. These requirements are applied during refueling operations 
    by Technical Specification 3.9.4, Refueling Operations, Containment 
    Building Penetrations. Technical Specification 3.9.4 is applicable in 
    Mode 6 and establishes containment closure vice CONTAINMENT INTEGRITY 
    during CORE ALTERATIONS and movement of irradiated fuel within 
    containment. Containment closure means that all potential release paths 
    are closed or capable of being closed to provide an atmospheric 
    pressure, ventilation barrier. Since there is no potential for 
    containment pressurization, establishment of a pressure tight boundary 
    is not required.
        As a part of the containment closure requirements of Technical 
    Specification 3.9.4, the Containment Equipment Hatch inside door must 
    be installed with a minimum of four bolts. In addition, each 
    penetration providing direct access from the containment atmosphere to 
    the outside atmosphere must be closed by either an isolation valve, a 
    blind flange, or a manual valve, or must be capable of being closed by 
    an OPERABLE automatic containment isolation valve.
        The proposed changes will modify Technical Specification 3/4.9.4 to 
    permit the use of an equivalent closure device as an alternative to 
    installation of the inner door with a minimum of four bolts to provide 
    containment closure for the Containment Equipment Hatch. The proposed 
    change will also modify Technical Specification 3.9.4 to permit the use 
    of an equivalent method for containment closure for containment 
    penetrations providing direct access from the containment to the 
    outside atmosphere as an alternate method to closure by an isolation 
    valve, blind flange, or manual valve. Any alternate method used will be 
    designed, fabricated, installed, tested, and utilized in accordance 
    with established procedures to ensure that it is capable of providing 
    containment closure during a fuel handling accident to prevent the 
    release of fission product radioactivity to the environment. Because 
    the proposed technical specifications must provide equivalent 
    containment closure, these changes will not increase the consequences 
    of an accident previously evaluated.
        Based upon the above, the proposed changes do not increase the 
    probability or the consequences of an accident previously evaluated.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed changes do not require any change in the operation of 
    the plant. The proposed changes will permit the use of an equivalent 
    method to achieve containment closure for the Containment Equipment 
    Hatch or for individual containment penetrations that provide direct 
    access to the outside atmosphere. However, any equivalent method used 
    will be designed, fabricated, installed, tested, and utilized in 
    accordance with established procedures to ensure that the closure 
    method meets design requirements.
        Based upon the above, these changes will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will not involve a significant reduction in a margin of safety.
        The proposed change will not affect the existing analysis that 
    forms the basis for the Technical Specifications, and does not violate 
    Technical Specification and Updated Final Safety Analysis Report 
    (UFSAR) requirements. The proposed change will not affect any design or 
    functional requirements of the containment, the Containment Equipment 
    Hatch, or containment penetrations or any conditions or assumptions of 
    the applicable safety analyses.
        Based upon the above, the proposed changes will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Project Director: Robert A. Capra.
    
    Southern California Edison Company, et al., Docket No. 50-362, San 
    Onofre Nuclear Generating Station, Unit No. 3, San Diego County, 
    California
    
        Date of amendment request: September 22, 1998.
        Description of amendment request: The proposed amendment would 
    modify the Technical Specifications (TS) to change the parameter used 
    to establish and remove the bypasses for high reactor power trips. The 
    parameter would be changed from the current ``THERMAL POWER'' to 
    logarithmic power. This amendment was processed on San Onofre Nuclear 
    Generating Station (SONGS) Unit 2 under emergency circumstances to 
    allow resumption of power operations, and is being processed under 
    normal notice circumstances on SONGS Unit 3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change to Technical Specification (TS) 3.3.1 does not 
    adversely impact structure, system, or component design or operation in 
    a manner which would result in a change in the frequency of occurrence 
    of accident initiation. The reactor trip bypass and automatic enable 
    functions are not accident initiators. Consequently, the proposed TS 
    change will not significantly increase the probability of accidents 
    previously evaluated. Clarifying the input process variable of the 
    operating bypasses and automatic bypass removals of the affected 
    reactor trips does not alter the setpoint nor the manner of operation 
    of the operating bypasses and automatic bypass removals. Therefore, the 
    consequences of previously evaluated accidents remain unchanged.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        No new or different accidents result from clarifying the input 
    process variable of the operating bypasses and automatic bypass 
    removals of the affected reactor trips. The results of previously 
    performed accident analyses remain valid. Therefore, this amendment 
    request does not create the possibility of a new or different kind of 
    accident.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed change does not alter the setpoint nor the manner of 
    operation of the operating bypasses and automatic bypass removals of 
    the affected reactor trips. The change merely replaces the 
    identification of the input process variable with the appropriate 
    identification of power. Therefore, this amendment request does not 
    involve a significant reduction in any margin of safety.
    
    [[Page 56260]]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: Douglas K. Porter, Esquire, Southern 
    California Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: August 31, 1998.
        Description of amendment request: The proposed amendment would 
    revise the cold overpressure mitigation curves in Technical 
    Specification (TS) Figure 3.4-4. This change would account for the TS 
    maximum allowable power-operated relief valve setpoint changes 
    associated with the new Model Delta 94 steam generator operating 
    parameters.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The current pressurizer maximum allowable Power Operated Relief 
    Valve (PORV) setpoints, provided by the Cold Overpressure Mitigation 
    System (COMS) curves (Figure 3.4-4) of Technical Specification 3.4.9.3, 
    are nonconservative for application with the new Delta 94 Replacement 
    Steam Generators. The South Texas Project Cold Overpressure Event has 
    been re-analyzed as a result of changed operating parameters due to 
    installation of new Delta 94 Steam Generators. The re-analysis 
    determined that maximum allowable PORV setpoint required decreases to 
    ensure that the Cold Overpressure Mitigation System (COMS) continued to 
    provide design basis low temperature overpressure protection with Delta 
    94 Steam Generators. New COMS curves have been developed and are to be 
    incorporated into Technical Specification 3.4.9.3 by this change 
    request. Since the proposed COMS curves result in maximum allowable 
    PORV setpoint decreases to account for the changed Delta 94 Steam 
    Generator operating parameters, these curves are more conservative than 
    the existing COMS curves utilized for Model E Steam Generators. 
    Therefore, application of these proposed COMS curves for a unit with 
    Model E or Delta 94 Steam Generators ensures compliance with the 
    original design basis of the Cold Overpressure Mitigation System for 
    the South Texas Project.
        This proposed change is based on a re-analysis which accounts for 
    changed operating parameters associated with the Delta 94 Replacement 
    Steam Generators. Reflecting actual operating parameters and adjusting 
    the maximum allowable PORV setpoints, as necessary, in the conservative 
    direction has no adverse effect on the probability or consequences of 
    an accident previously evaluated. Therefore, the proposed change does 
    not involve a significant increase in the probability or consequences 
    of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed PORV maximum allowable setpoint changes do no create 
    any new operating conditions or modes. The proposed change only revises 
    the maximum allowable PORV setpoint curves for the Cold Overpressure 
    Mitigation System to account for the revised operating parameters 
    associated with Delta 94 Steam Generators. The actions of this system 
    continue to be performed in accordance with existing requirements, 
    which are sufficient to ensure plant safety is maintained.
        The proposed change is the result of a re-analysis of a previously 
    evaluated accident. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed change reflects the revised operating parameters 
    associated with the new Delta 94 Steam Generators. The revised COMS 
    curves are the result of a re-analysis of the COMS analysis performed 
    to ensure the margin of safety is not reduced with Delta 94 Steam 
    Generators. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869.
        NRC Project Director: John N. Hannon.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, Ohio
    
        Date of amendment request: August 31, 1998.
        Description of amendment request: The proposed amendment would 
    modify Technical Specification Surveillance Requirement 3.6.1.3.4 to 
    permit removal of the inclined fuel transfer system primary containment 
    blind flange while primary containment integrity is required.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        (1) The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change permits removal of the blind flange on the 
    Inclined Fuel Transfer System (IFTS) when primary containment 
    operability is required in Modes 1, 2 and 3. This will permit operation 
    of IFTS when the plant is operating. This aspect of the containment 
    structure does not directly interface with the reactor coolant pressure 
    boundary. The removal of this blind flange does not involve 
    modifications to plant systems or design parameters that could 
    contribute to the initiation of any accidents previously evaluated. 
    Operation of IFTS is unrelated to the operation of the reactor, and 
    there is no aspect of IFTS operation that could lead to or contribute 
    to the probability of occurrence of an accident previously evaluated. 
    Removal of the blind flange and operation of IFTS does not result in 
    changes to procedures that could impact the probability of occurrence 
    of an accident.
        With respect to consequences, the function of the containment is to
    
    [[Page 56261]]
    
    mitigate the radiological consequences of a loss of coolant accident 
    (LOCA) or other postulated events that could result in radiation 
    release from the fuel inside containment. The pressure and temperature 
    transient resulting from a design basis loss of coolant accident (LOCA) 
    is considered the primary challenge to the integrity of the 
    containment. While the proposed change does not change the plant 
    design, it does permit alteration of the containment boundary for the 
    IFTS penetration. Altering the containment boundary in this case 
    (removing the blind flange) results in some IFTS components possibly 
    seeing a containment pressure rise should a LOCA occur. The thermal and 
    mechanical load requirements do not appreciably change as a result of 
    such a small pressure increase (peak post-accident pressure 
    (Pa) of 7.8 psig). The IFTS components will be more than 
    adequate and capable of withstanding the Design Basis LOCA and 
    associated loads prior to implementation of this amendment. Therefore, 
    they are considered an acceptable barrier to prevent uncontrolled 
    release of post-accident fission products for this proposed change.
        The proposed change required examination of two potential leakage 
    pathways. The larger is the transfer tube itself, the other, much 
    smaller one, is the drain piping. It is clear that the gate valve at 
    the bottom of the transfer tube is always water sealed and maintained 
    so by the submergence of the water in the transfer tube and in the Fuel 
    Handling Building Fuel Transfer Pool. The height of this water seal is 
    greater than that necessary to prevent leakage from the bottom of the 
    transfer tube during accidents that result in the calculated peak post-
    accident pressure (Pa). The potential leakage pathway from 
    the drain piping which attaches to the transfer tube will be isolated 
    if required, via administrative controls on the drain piping isolation 
    valve. Additionally, the drain piping isolation valve will be added to 
    the Primary Containment Leakage Rate Testing Program (Specification 
    5.5.12) to ensure that leakage past this valve will be maintained 
    consistent with the leakage rate assumptions of the accident analysis. 
    Due to the test methodology, the portion of the large transfer tube 
    piping outboard of the blind flange (the portion of the tube which 
    becomes exposed to containment air during the draining portion of the 
    IFTS operation) will also be part of the leakage rate test boundary and 
    will therefore also be tested with air. Therefore, no unidentified 
    leakage paths will exist from the piping and components that are 
    outboard of the blind flange, and the leakage rate assumptions of the 
    accident analysis will be maintained.
        Therefore, the proposed change does not result in a significant 
    increase in the probability or the consequences of previously evaluated 
    accidents.
        (2) The proposed change would not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed change consists of the removal of a passive component 
    which is not part of the primary reactor coolant pressure boundary nor 
    involved in the operation or shutdown of the reactor. Being passive, 
    its presence or absence does not affect any of the parameters or 
    conditions that could contribute to the initiation of any incidents or 
    accidents that are created from loss of coolant or positive reactivity. 
    Re-aligning the boundary of the primary containment to include portions 
    of the IFTS is also passive in nature and therefore has no influence 
    on, nor does it contribute to the possibility of a new or different 
    kind of incident, accident or malfunction from those previously 
    analyzed. Furthermore, operation of IFTS is unrelated to the operation 
    of the reactor and there is no mishap in the process that can lead or 
    contribute to the possibility of losing any coolant in the reactor or 
    introducing the chance for positive or negative reactivity or other 
    accidents different from and not bounded by those previously evaluated.
        Therefore, the proposed change does not result in creating the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        (3) The proposed change will not involve a significant reduction in 
    the margin of safety.
        The proposed change involves the re-alignment of the primary 
    containment boundary by removing the blind flange which is a passive 
    component. The margin of safety that has the potential of being 
    impacted by the proposed change involves the dose consequences of 
    postulated accidents which are directly related to potential leakage 
    through the primary containment boundary. The potential leakage 
    pathways due to the proposed change have been reviewed, and leakage can 
    only occur from the administratively controlled IFTS transfer tube 
    drain piping. An individual will be designated to provide timely 
    isolation of this drain piping during the durations of time when this 
    proposed change is in effect. The conservatively calculated dose which 
    might be received by the designated individual while isolating the 
    drain piping is less than or equal to 1.9 rem, well within the 
    guidelines of General Design Criterion 19. Furthermore, the drain 
    piping isolation valve will be added into the Primary Containment 
    Leakage Rate Testing Program (Specification 5.5.12) to ensure that 
    leakage from the piping and components located outboard of the blind 
    flange will be maintained consistent with the leakage rate assumptions 
    of the accident analysis. Therefore, the dose consequences of an event 
    would be unchanged, and the associated margin of safety would also be 
    unchanged.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Stuart A. Richards.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, Ohio
    
        Date of amendment request: September 3, 1998.
        Description of amendment request: The proposed amendment would 
    permit an Emergency Diesel Generator (EDG) Technical Specification (TS) 
    Action Completion Time of up to 14 days for a Division 1 or 2 EDG and 
    allow performance of the EDG 24-hour TS surveillance requirement test 
    in modes 1 and 2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed Technical Specification changes do not significantly 
    increase the probability of occurrence of a previously evaluated 
    accident because the standby
    
    [[Page 56262]]
    
    Emergency Diesel Generators (EDGs), including the High Pressure Core 
    Spray diesel generator, are not initiators of previously evaluated 
    accidents. The EDGs mitigate the consequences of previously evaluated 
    accidents involving a loss of offsite power. The proposed changes to 
    the Technical Specification Action Completion Times do not affect any 
    of the assumptions used in the deterministic or Probabilistic Safety 
    Analysis (PSA).
        The proposed Technical Specification changes will continue to 
    ensure the EDGs perform their function when called upon. Extending the 
    Technical Specification Completion Times to 14 days and allowing the 
    performance of the EDG 24-hour run test in either Modes 1 or 2 does not 
    affect the design of the EDGs, the operational characteristics of the 
    EDGs, the interfaces between the EDGs and other plant systems, the 
    function, or the reliability of the EDGs. Thus, the EDGs will be 
    capable of performing their accident mitigation function and there is 
    no impact to the radiological consequences of any accident analysis.
        To fully evaluate the effect of the EDG Completion Time extension, 
    PSA methods and deterministic analysis were utilized. The results of 
    this analysis show no significant increase in the Core Damage 
    Frequency. The proposed changes remain bounded by the Core Damage 
    Frequency identified in the Individual Plant Examination.
        The Configuration Risk Management Program (CRMP) is an 
    administrative program that assesses risk based on plant status. Adding 
    the requirement to implement the CRMP for Technical Specification 3.8.1 
    requires the consideration of other measures to mitigate consequences 
    of an accident occurring while an EDG is inoperable.
        The proposed change will not alter the operation of any plant 
    equipment assumed to function in response to an analyzed event or 
    otherwise increase its failure probability. Therefore, this change does 
    not involve a significant increase in the probability or consequences 
    of any accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        This proposed change does not change the design, configuration, or 
    method of operation of the plant. The proposed activity involves a 
    change to the allowed plant mode for the performance of specific 
    Technical Specification surveillance requirements. No physical or 
    operational changes to the EDGs or supporting systems are made by this 
    activity. Since the proposed changes do not involve a change to the 
    plant design or operation, no new system interactions are created by 
    this change. The proposed Technical Specification changes do not 
    produce any parameters or conditions that could contribute to the 
    initiation of accidents different from those already evaluated in the 
    Updated Safety Analysis Report.
        The proposed changes only address the methods used to ensure EDG 
    reliability. Thus, the proposed Technical Specification change does not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed changes do not affect the Limiting Conditions for 
    Operation or their Bases that are used in the deterministic analysis to 
    establish any margin of safety. PSA evaluations were used to evaluate 
    these changes, and these evaluations determined that the changes are 
    either risk neutral or risk beneficial. The proposed activity involves 
    changes to certain Completion Times and to the allowed plant mode for 
    the performance of specific Technical Specification Surveillance 
    Requirements. The proposed change remains bounded by the existing 
    Surveillance Requirement Completion Times and therefore has no impact 
    to the margins of safety.
        The proposed change does not involve a change to the plant design 
    or operation, and thus does not affect the design of the EDGs, the 
    operational characteristics of the EDGs, the interfaces between the 
    EDGs, and other plant systems, or the function or reliability of the 
    EDGs. Because EDG performance and reliability will continue to be 
    ensured by the proposed Technical Specification changes, the proposed 
    changes do not result in a reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Stuart A. Richards.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, Ohio
    
        Date of amendment request: September 9, 1998.
        Description of amendment request: The proposed license amendment 
    concerns hydrostatic (water) testing of containment isolation valves in 
    the Feedwater System lines. The proposed technical specification change 
    stipulates that water leakage from the feedwater motor-operated 
    containment isolation valves will be added into the Primary Coolant 
    Sources Outside of Containment Program (Technical Specification 5.5.2), 
    and therefore the feedwater check valves do not need to be included in 
    the hydrostatic test program addressed by Surveillance Requirement 
    3.6.1.3.11. The proposed testing change is based on design and 
    licensing basis changes being implemented to improve functioning of the 
    Feedwater Leakage Control System.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        (1) This proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        It is proposed that water leakage from the Feedwater motor-operated 
    containment isolation valves will be added into the Primary Coolant 
    Sources Outside Containment Program (Technical Specification 5.5.2), 
    and therefore the Feedwater lines do not need to also be included in 
    the hydrostatic test program addressed by Surveillance Requirement 
    3.6.1.3.11. The proposed testing change is based on design/licensing 
    basis changes being implemented to improve functioning of the Feedwater 
    Leakage Control System. The proposed design change will provide 
    Feedwater Leakage Control System seal water directly to the bonnets and 
    seats of the motor operated gate valves in the Feedwater lines, and 
    allow for power to the valves to be provided from redundant power 
    supplies.
        The proposed changes do not increase the probability of occurrence 
    of an accident previously evaluated because the Feedwater Leakage 
    Control System is not an initiator of a previously evaluated accident. 
    The Feedwater Leakage Control System is used to
    
    [[Page 56263]]
    
    mitigate the consequences of an event that has already been initiated 
    due to some other cause, specifically a design basis Loss of Coolant 
    Accident (LOCA). Therefore, changes to the design and testing on the 
    Feedwater Leakage Control System have no impact on the probability of 
    occurrence of an accident previously evaluated. The Feedwater Leakage 
    Control System is a manually initiated system, and the probability of 
    an inadvertent initiation remains unchanged from that previously 
    reviewed, so the possibility of a loss of feedwater transient is not 
    increased.
        The proposed changes do not significantly increase the radiological 
    consequences of an accident previously evaluated, because the Feedwater 
    lines will continue to be isolated following a LOCA either inside or 
    outside of containment. For a line break outside of containment, the 
    check valves will provide the necessary short-term closure function to 
    prevent significant loss of reactor coolant inventory, as currently 
    stated in Updated Safety Analysis Report (USAR) Section 
    6.2.4.2.2.1.a.1. The third (gate) valves in the Feedwater line will 
    also be available to provide the long-term, high integrity leakage 
    protection. The check valves Code Class 1 closure function will be 
    verified at an appropriate frequency by performance of an exercise 
    closed (EC) test comprised of a visual inspection of the internals of 
    the valves, in accordance with the Inservice Testing Program. The 
    radiological consequences of such a line break outside of containment 
    event are not significant, as there is no postulated fuel damage.
        For a line break inside of containment (a design basis LOCA event), 
    the majority of the currently reviewed and accepted licensing basis is 
    being maintained. Design changes are being implemented to improve the 
    functioning of the Feedwater Leakage Control System. The redundant 
    subsystems will be piped to the bonnets of the third, high integrity 
    valves in the Feedwater lines (the gate valves) to provide a more rapid 
    and effective seal on the stem, bonnet and flexible wedge seats. Water 
    leakage from the stem, bonnets and seats of the gate valves will be 
    addressed through controls imposed by Technical Specification 5.5.2, 
    ``Primary Coolant Sources Outside Containment.'' The doses from such 
    water leakage are accounted for in the radiological dose calculations. 
    Since the leakage from the Feedwater lines is accounted for by the 
    Primary Coolant Sources Outside Containment Program, there is no need 
    to include the water test results of the Feedwater lines into the 
    Surveillance Requirement 3.6.1.3.11 leak test totals.
        The branch lines off of the Feedwater lines will also be addressed 
    either through the Primary Coolant Sources Outside Containment Program 
    (Technical Specification 5.5.2) or through additional Appendix J air 
    leak rate test requirements (Technical Specification Surveillance 
    Requirement 3.6.1.1.1 and Specification 5.5.12, ``Primary Containment 
    Leakage Rate Testing Program''). The new test methods for these lines 
    do not impact the existing radiological dose calculations, since the 
    existing leakage limits of the leak rate test programs are not changed 
    by the proposal.
        The design changes associated with the Feedwater Leakage Control 
    System will continue to satisfy licensing/design criteria for this 
    piping to an equivalent degree as the current design. The minor 
    exception is where the two Feedwater Leakage Control subsystems tie in 
    to the bonnets of the gate valves, and this constitutes only a 
    separation issue. Since the Feedwater Leakage Control System piping at 
    this juncture is Code Class 2, break excluded, and protected from pipe 
    whips and jet impingements, it is considered to be acceptable.
        Addition of the provisions for an alternate power supply to be 
    provided to the gate valves (if necessary following a LOCA event) will 
    improve the probability of closure of these high integrity valves 
    without creating an electrical separation concern. A separation concern 
    will not be created since the supply circuitry from the alternate power 
    source will be a permanent modification, and physical and electrical 
    separation between electrical divisions will be maintained by employing 
    two features:
        1. Normally open, fused disconnect switches at both ends of the 
    circuit, and
        2. Fuses normally stored out of the circuit.
        Based on the discussions above, it is concluded that neither the 
    probability nor the consequences of previously evaluated accidents are 
    significantly increased as a result of the proposed changes to the 
    Technical Specifications and to the licensing bases for the Feedwater 
    penetrations.
        (2) This proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The Feedwater Leakage Control System was developed specifically to 
    mitigate the consequences of a design basis LOCA inside the 
    containment. The system itself and the proposed changes do not produce 
    parameters or conditions that could contribute to the initiation of 
    accidents different than those already evaluated in the Updated Safety 
    Analysis Report. The proposed changes are intended to improve the 
    functioning of the Feedwater Leakage Control System should it be called 
    upon following a LOCA. The changes affect mitigation of that previously 
    evaluated event.
        In other plant conditions, including normal operation, the system 
    is not activated and cannot induce events. Thus, the proposed amendment 
    does not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        (3) This proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed changes only affect the methods used to ensure 
    Feedwater Leakage Control System performance and reliability, and 
    clarification of the licensing/design basis of the system. The new 
    proposed Note in Surveillance Requirement 3.6.1.3.11 clarifies that the 
    water leakage from the Feedwater lines does not need to be counted in 
    two separate leak test programs. The Primary Coolant Sources Outside 
    Containment Program (Technical Specification 5.5.2) will ensure that 
    leakage from the Feedwater lines is minimized, and accounted for in an 
    appropriate fashion in the radiological does calculations. Leak rate 
    testing on the branch lines off of the Feedwater lines will also be 
    controlled and limited by existing acceptance criteria for plant 
    programs that protect the assumptions of the radiological dose 
    calculations. Therefore, the margin of safety provided in the Perry 
    Nuclear Power Plant dose calculations will remain unchanged.
        The majority of the existing licensing basis, and therefore the 
    margins of safety, are maintained by this proposal. The items that are 
    changed are done so to improve the reliability of the system or for an 
    administrative clarification. The Feedwater Leakage Control System 
    Technical Specification itself (Technical Specification 3.6.1.8) does 
    not need revision. The design changes will maintain the existing 
    licensing/design criteria, with the minor exception of divisional 
    separation at the point that the two divisions have to be piped into 
    the bonnets of the third (gate) valve. Since the piping at this 
    junction point is Code Class 2, break excluded, and protected from pipe 
    whips and jet impingements, it is considered to be acceptable. It will 
    not lead to a significant reduction in a margin of safety. The manually 
    initiated divisional cross-tie will not create an electrical separation 
    concern. The alternate power supply provision will be a permanent
    
    [[Page 56264]]
    
    modification, and physical and electrical separation between electrical 
    divisions will be maintained.
        Based on the above discussions, the proposed license amendment is 
    concluded to not result in a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Stuart A. Richards.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Duke Energy Corporation , Docket Nos. 50-269, 50-270, and 50-287, 
    Oconee Nuclear Station, Units 1, 2, and 3, Oconee County, South 
    Carolina
    
        Date of amendment request: September 17, 1998.
        Description of amendment request: The proposed amendments would 
    allow a revision to the Oconee Updated Final Safety Analysis Report 
    that addresses potential plant conditions that could occur during 
    engineered safeguards functional tests of the emergency electrical 
    system. These tests are planned to be performed on Unit 3 in November 
    1998, with Unit 3 in the cold shutdown condition, and Units 1 and 2 
    operating at power. If an actual loss-of-coolant accident with loss of 
    offsite power were to occur on Unit 1 or 2, simultaneously with test 
    initiation on Unit 3, the Emergency Power System would be placed in a 
    condition outside the present design basis. This involves an unreviewed 
    safety question that requires NRC approval before implementation of the 
    tests.
        Date of publication of individual notice in Federal Register: 
    September 30, 1998 (63 FR 52304).
        Expiration date of individual notice: October 30, 1998.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
    GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey
    
        Date of amendment request: September 19, 1998.
        Description of amendment request: The amendment would revise 
    Section 5.4.8 of the Oyster Creek Nuclear Generating Station Updated 
    Final Safety Analysis Report (UFSAR) such that it incorporates the use 
    of a freeze seal as a temporary part of the reactor coolant pressure 
    boundary.
        Date of publication of individual notice in Federal Register: 
    September 30, 1998 (63 FR 52307).
        Expiration date of individual notice: October 30, 1998.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Units 1 and 2, Goodhue County, 
    Minnesota
    
        Date of amendment requests: January 29, 1997, as supplemented 
    February 11, 12, March 7, 10, 11, 19, 20, April 29, June 30, and July 
    10, 1997, June 20, June 22, July 24 and September 15, 1998.
        Brief description of amendment request: The proposed amendments 
    would change the design basis of the cooling water system emergency 
    intake line flow capacity. The licensee determined through testing that 
    the emergency intake line flow capacity was less than the design value 
    stated in the Updated Safety Analysis Report. The proposed changes 
    reflect the use of operator actions to control cooling water system 
    flow following a seismic event. The proposed changes also reclassify 
    the intake canal for use during a seismic event, which would be an 
    additional source of cooling water during a seismic event.
        Date of publication of individual notice in Federal Register: 
    October 1, 1998 (63 FR 52772).
        Expiration date of individual notice: November 2, 1998.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: October 14, 1997, as supplemented July 
    23, 1998.
        Description of amendment request: The amendment would update the 
    Technical Specifications to provide for installation of additional 
    racks to increase spent fuel storage capacity, and to correct the 
    maximum exposure dependent, infinite lattice multiplication factor for 
    fuel bundles.
        Date of publication of individual notice in Federal Register: 
    August 24, 1998 (63 FR 45096).
        Expiration date of individual notice: September 23, 1998.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch 
    Nuclear Plant, Units 1 and 2, Appling County, Georgia
    
        Date of amendment request: August 8, 1997, as supplemented by 
    letters dated March 9, May 6, July 6, July 31, September 4, and 
    September 11, 1998, and advanced information related to the application 
    submitted April 17, 1998.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications to accommodate an increase in the 
    maximum licensed thermal power level from 2558 megawatts thermal (MWt) 
    to 2736 MWt.
        Date of publication of individual notice in Federal Register: 
    October 6, 1998 (63 FR 53730).
        Expiration date of individual notice: November 5, 1998.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia.
    
    [[Page 56265]]
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: September 4, 1998.
        Description of amendment request: The amendment would revise the 
    Technical Specifications to reflect an increase in the spent fuel 
    storage capacity.
        Date of publication of individual notice in Federal Register: 
    October 1, 1998. (63 FR 52774)
        Expiration date of individual notice: November 2, 1998.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendment: June 13, 1995, as supplemented 
    by letters dated August 16, 1995, June 9, 1998, and September 6, 1998.
        Brief description of amendment: These amendments revise TS 3.5.1, 
    ``Safety Injection Tanks (SITs)--Operating,'' and TS 3.5.2, ``Safety 
    Injection Tanks--Shutdown,'' to extend the allowed outage times for the 
    SITs.
        Date of issuance: October 2, 1998.
        Effective date: October 2, 1998.
        Amendment No.: 118.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendment revised the Technical Specifications.
        Date of initial notice in Federal Register: October 25, 1995 (60 FR 
    54715)
        The June 9, 1998, and September 6, 1998, letters provided 
    additional clarifying information and do not change the initial no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: June 12, 1997, as supplemented 
    by letter dated August 27, 1998. The August 27, 1998, supplemental 
    letter provided clarifying information only, and did not change the 
    initial no significant hazards consideration determination.
        Brief description of amendment: This amendment changes the 
    description of the Harris Nuclear Plant Operations organization in TS 
    6.0, ``Administrative Controls.''
        Date of issuance: October 7, 1998.
        Effective date: October 7, 1998.
        Amendment No: 83.
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 30, 1997 (62 FR 
    40847).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 7, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois
    
    Docket Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 
    and 2, Will County, Illinois
    
        Date of application for amendments: December 30, 1997.
        Brief description of amendments: The amendments change the 
    Technical Specifications for the condensate storage tank (CST) level 
    and the automatic auxiliary feedwater pump switchover from the suction 
    of the CST to the essential service water system.
        Date of issuance: October 6, 1998.
        Effective date: October 6, 1998.
        Amendment Nos.: 104; 104 & 96; 96.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 25, 1998. (63 
    FR 9596)
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 6, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 
    1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: May 18, 1998.
        Brief description of amendments: The amendments will change several 
    Technical Specification (TS) values to reflect design values. These TS 
    values affect (1) 125/250 volts direct current (Vdc) electrolyte 
    temperature; (2) control rod drive accumulator pressure; (3) standby 
    liquid control solution temperature; (4) ultimate heat sink minimum 
    water level; (5) shutdown
    
    [[Page 56266]]
    
    suppression chamber level (Quad Cities only); and (6) a degraded 
    voltage setpoint (Quad Cities only).
        Date of issuance: October 8, 1998.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: Dresden 169 & 164; Quad Cities 181 & 179.
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 17, 1998 (63 FR 
    33105).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 8, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
    
    Duke Energy Corporation, et al., Docket No. 50-414, Catawba Nuclear 
    Station, Unit 2, York County, South Carolina
    
        Date of application for amendment: August 6, 1998.
        Brief description of amendment: The amendment deletes Surveillance 
    Requirement 4.8.1.1.2.i.2, regarding diesel fuel oil system pressure 
    testing, from the Technical Specifications on the basis that the staff 
    had previously approved alternative surveillance based on Code Case N-
    498-1 of the American Society of Mechanical Engineers.
        Date of issuance: September 28, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment No.: 164.
        Facility Operating License No. NPF-52: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1998 (63 FR 
    43962).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 28, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    Duke Energy Corporation, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: October 22, 1996, as 
    supplemented by letters dated March 19, July 6, and September 15, 1998.
        Brief description of amendments: The amendments allow continued 
    plant operation at elevated Containment Lower Compartment temperatures 
    between 125  deg.F and 135  deg.F for a period not to exceed 72 
    cumulative hours per calendar year.
        Date of issuance: September 28, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: Unit 1-183; Unit 2-165.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6574).
        The March 19, July 6, and September 15, 1998, submittals provided 
    clarifying information that did not change the scope of the October 22, 
    1996, application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 28, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina.
    
    GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey
    
        Date of application of amendment: July 21, 1998.
        Brief description of amendment: The amendment permits an 
    alternative to the requirement to perform Control Rod Drive scram time 
    testing with the reactor pressurized prior to resuming power operation. 
    The change permits: (1) scram time testing with the reactor 
    depressurized prior to resuming operation, and (2) a second scram time 
    test with the reactor pressure above 800 psig, prior to exceeding 40% 
    reactor power.
        Date of Issuance: October 1, 1998.
        Effective date: October 21, 1998, to be implemented within 30 days.
        Amendment No.: 198.
        Facility Operating License No. DPR-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 12, 1998 (63 FR 
    43204).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated October 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    GPU Nuclear, Inc., et al., Docket No. 50-289, Three Mile Island Nuclear 
    Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: March 23, 1998, as supplemented 
    June 30, 1998.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.1.2, to incorporate new pressure/temperature 
    limits for reactor vessel pressurization heatup, cooldown, and 
    inservice leak and hydrostatic test.
        Date of issuance: October 5, 1998.
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 208.
        Facility Operating License No. DPR-50: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 22, 1998 (63 FR 
    19970). The June 30, 1998, submittal provided additional information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 5, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of application for amendment: April 15, 1998.
        Brief description of amendment: The amendment revises the Technical 
    Specifications by updating the existing pressure-temperature curves 
    with new curves with values from 18 to 32 effective full power years. 
    Applicable surveillance requirements are also revised to reflect 
    operation with the new curves.
        Date of issuance: October 1, 1998.
        Effective date: October 1, 1998.
        Amendment No.: 224.
        Facility Operating License No. DPR-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 6, 1998 (63 FR 
    25110).
    
    [[Page 56267]]
    
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, IA 52401.
    
    Illinois Power Company, Docket No. 50-461, Clinton Power Station, Unit 
    1, DeWitt County, Illinois
    
        Date of application for amendment: May 20, 1998, as supplemented 
    July 17 and August 6, 1998.
        Brief description of amendment: The amendment provides for 
    automatic operation of a new emergency reserve auxiliary transformer to 
    provide power to the plant 4.16-kV buses from the offsite 138-kV 
    transmission network.
        Date of issuance: October 1, 1998.
        Effective date: October 1, 1998.
        Amendment No.: 116.
        Facility Operating License No. NPF-62: The amendment authorized 
    revision of the Updated Safety Analysis Report.
        Date of initial notice in Federal Register: June 4, 1998 (63 FR 
    30519).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, IL 61727.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket 
    Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit Nos. 2 
    and 3, York County, Pennsylvania
    
        Date of application for amendments: May 23, 1997, as supplemented 
    by letter dated September 11, 1998. The September 11, 1998, letter 
    provided the typed TS pages that did not change the Nuclear Regulatory 
    Commission staff's proposed no significant hazards consideration 
    determination.
        Brief description of amendments: The proposed amendments would 
    revise the Technical Specifications TSs to exclude the Main Steam 
    Isolation Valves leakage from the total Type B and Type C local leak 
    rate test results.
        Date of issuance: October 1, 1998.
        Effective date: The amendments are effective as of the date of 
    issuance, and are to be implemented within 30 days from the date of 
    their issuance.
        Amendments Nos.: 223 and 227.
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 2, 1998 (62 FR 
    35852).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket 
    Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit Nos. 2 
    and 3, York County, Pennsylvania
    
        Date of application for amendments: May 1, 1998, as supplemented by 
    letter dated September 11, 1998.
        Brief description of amendments: These amendments revise the 
    technical specifications to delete the requirements for functional 
    testing of safety relief valves during each unit startup.
        Date of issuance: October 5, 1998.
        Effective date: As of the date of issuance and is to be 
    implemented, Unit 2, prior to October 1998 refueling outage and Unit 3, 
    prior to October 1999 refueling outage.
        Amendments Nos.: 224 and 228.
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 29, 1998 (63 FR 
    40559).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 5, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket 
    Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit Nos. 2 
    and 3, York County, Pennsylvania
    
        Date of application for amendments: March 20, 1998, as supplemented 
    by letters dated June 26, August 11, and September 14, 1998. The August 
    11 an September 14 letters provided clarifying information that did not 
    change the initial proposed no significant hazards consideration 
    determination.
        Brief description of amendments: These amendments would revise the 
    Technical Specifications to permit incorporation of end-of-cycle 
    recirculation pump trip systems.
        Date of issuance: October 5, 1998.
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendments Nos.: 225 and 229.
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 29, 1998 (63 FR 
    40558).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 5, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: March 24, 1997, as supplemented 
    September 4, 1998.
        Brief description of amendments: These amendments approve the 
    deletion of the Drywell and Suppression Chamber Purge System 
    operational time limit, removal of a footnote regarding 1-inch and 2-
    inch valves, and the addition of a surveillance requirement ensuring 
    the purge system large supply and exhaust valves are closed as 
    required.
        Date of issuance: October 1, 1998.
        Effective date: Units 1 and 2, As of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 130 and 91.
        Facility Operating License Nos. NPF-39 and NPF-85: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 4, 1997 (62 FR 
    30643).
        The September 4, 1998, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
    
    [[Page 56268]]
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County , New York
    
        Date of application for amendment: November 13, 1997.
        Brief description of amendment: The amendment changes the Technical 
    Specifications by increasing the minimum test frequency for main 
    turbine stop valves.
        Date of issuance: October 5, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 182.
        Facility Operating License No. DPR-64: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 15, 1998 (63 FR 
    38203).
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: May 13, 1998.
        Brief description of amendment: This amendment revises Technical 
    Specification (TS) 3/4.10.8, ``Inservice Leak and Hydrostatic 
    Testing,'' to delete the requirement for an operable High Drywell 
    Pressure trip function. Specifically, TS 3.10.8.a is being revised to 
    remove the reference to the Secondary Containment Isolation Actuation 
    Instrumentation trip function 2.b.
        Date of issuance: October 1, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 112.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 1, 1998 (63 FR 
    35994).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: December 31, 1997, as supplemented June 
    30, August 6, August 18, and August 27, 1998.
        Brief description of amendments: The amendments revised TS 2.1 
    (Safety Limits), 2.2 (Limiting Safety System Settings), and 3/4.2.5 
    (Departure from Nucleate Boiling Parameters) by including alternate 
    operating criteria to allow continued plant operation with a reduced 
    measured reactor coolant system flow rate, if necessary.
        Date of issuance: September 29, 1998.
        Effective date: September 29, 1998.
        Amendment Nos.: Unit 1--Amendment No. 97; Unit 2--Amendment No. 84.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4325).
        The additional information contained in the supplemental letters 
    dated June 30, August 6, August 18, and August 27, 1998, were 
    clarifying in nature and thus, within the scope of the initial notice 
    and did not affect the staff's proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 29, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit 1, Ottawa County, Ohio.
    
        Date of application for amendment: April 18, 1997, as supplemented 
    by letters dated October 10, 1997, and February 27 and September 8, 
    1998.
        Brief description of amendment: This amendment revises TS Section 
    3/4.7.6, ``Plant Systems--Control Room Emergency Ventilation System,'' 
    and the associated bases. Action statements have been added related to 
    the availability of the station vent normal range radiation monitoring 
    instrumentation. The bases have been modified consistent with these 
    changes.
        Date of issuance: October 5, 1998.
        Effective date: October 5, 1998.
        Amendment No.: 227.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 4, 1997 (62 FR 
    30646). The supplemental information submitted by letters dated October 
    10, 1997, and September 8, 1998, did not affect the proposed no 
    significant hazards consideration. However, the supplemental letter 
    dated February 27, 1998, included a new analysis of the issue of no 
    significant hazards consideration. Based on this, the Commission issued 
    a new proposed finding that the amendment involves no significant 
    hazards consideration (63 FR 25117). The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    October 5, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, OH 43606.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: August 8, 1997, as supplemented 
    by letters dated December 16, 1997, January 20, 1998, March 4, 1998, 
    March 17, 1998, June 29, 1998, and July 28, 1998.
        Brief description of amendment: The amendment revised Technical 
    Specification (TS) 3.7-2 to specify that the lift setting tolerance for 
    the main steam line safety valves is +3/-1 percent as-found and +/-1 
    percent as-left. The amendment also revised TS Table 2.2-1 to reduce 
    the sensor error for the pressurizer pressure-high trip.
        Date of issuance: October 2, 1998.
        Effective date: October 2, 1998, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 128.
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 17, 1997 (62 
    FR 66144).
        The December 16, 1997, January 20, 1998, March 4, 1998, March 17, 
    1998, June 29, 1998, and July 28, 1998, supplemental letters provided 
    additional clarifying information and did not change the initial no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated October 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Elmer Ellis Library, 
    University of Missouri, Columbia, Missouri 65201-5149.
    
    [[Page 56269]]
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: May 14, 1998, supplemented July 
    3, August 27, and October 1, 1998.
        Brief description of amendment: This amendment redefines the 
    pressure boundary for Westinghouse mechanical hybrid expansion joints 
    (HEJs) in sleeved steam generator tubes. TS 4.2 b, ``Steam Generator 
    Tubes,'' is changed to incorporate a length criterion to allow tubes 
    with degraded HEJ sleeves to remain in service if a minimum length of 
    the HEJ is free of flaws.
        Date of issuance: October 2, 1998.
        Effective date: October 2, 1998.
        Amendment No.: 139.
        Facility Operating License No. DPR-43: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 3, 1998 (63 FR 
    30269).
        The July 3, August 27, and October 1, 1998 submittals provided 
    clarifying information within the scope of the original Federal 
    Register notice and did not change the staff's initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    October 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, WI 54311-7001
    
        Dated at Rockville, Maryland, this 14th day of October 1998.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director Division of Reactor Projects--III/IV, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 98-28069 Filed 10-20-98; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
10/2/1998
Published:
10/21/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-28069
Dates:
October 2, 1998.
Pages:
56238-56269 (32 pages)
PDF File:
98-28069.pdf