X94-11026. Applications and Amendments to Facility Operating LicensesInvolving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 206 (Wednesday, October 26, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-11026]
    
    
    [[Page Unknown]]
    
    [Federal Register: October 26, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
     
    
    Applications and Amendments to Facility Operating 
    LicensesInvolving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from September 30, through October 14, 1994. The 
    last biweekly notice was published on October 12, 1994 (59 FR 51616).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By November 25, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request:  September 23, 1994
        Description of amendments request: The proposed amendments would 
    revise the Unit 2 Shutdown AC Sources Technical Specifications (TSs) to 
    allow a one-time extension from 7 to 14 days of the allowed outage time 
    (AOT) for the dedicated Class 1E emergency power source during the 
    upcoming Unit 2 1995 Refueling Outage (RFO-10). The proposed amendments 
    would also revise the Unit 1 Control Room Emergency Ventilation System 
    (CREVS) TSs to provide a one-time extension from 7 to 30 days of the 
    AOT for one train of the CREVS to be inoperable. As noted, these 
    extensions will be needed during the upcoming 1995 Unit 2 RFO-10 to 
    support the modifications scheduled for the onsite electrical 
    distribution system in response to the Station Blackout (SBO) Rule, 10 
    CFR 50.63, and the upgrade of No. 21 Emergency Diesel Generator 
    (EDG).The specific changes requested are:
        Unit 2 TSs 3.8.1.2 and 3.8.2.2 will include a footnote indicating 
    that the AOT for aligning an operable emergency diesel generator (EDG) 
    to provide power to the emergency busses within 14 days during the Unit 
    2 RFO-10.
        Unit 1 TS 3.7.6.1 will be modified to indicate that during the No. 
    21 EDG upgrade, the time to restore the No. 21 filter train of the air 
    conditioning unit to operable status may be extended to 30 days (for 
    loss of emergency power only) if: 1) A temporary diesel generator is 
    demonstrated to be available by starting it at least once per 7 days 
    and 2) if action 1 is not met, restore compliance with the action 
    within 7 days or be at least in hot standby within the next 6 hours and 
    in cold shutdown within the following 30 hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of issue of no significant hazards consideration 
    for each of the proposed changes, which is presented below:
        In relation to the requested changes to the Unit 2 TSs:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        Requiring one Class 1E Emergency Diesel Generator (EDG) to be 
    available for a shutdown unit ensures that AC power will be 
    available for a loss of offsite power event, a boron dilution event, 
    or a fuel handling incident. There is a very low probability that a 
    loss of offsite power will occur due to severe weather or 
    inadvertent damage to the switchyard during the 14-day period that 
    the temporary splice box is being installed and No. 12 EDG is out-
    of-service. The Calvert Cliffs offsite power supply is highly 
    redundant and has significant capability in withstanding severe 
    weather events, such as tornadoes. In addition, Calvert Cliffs 
    Emergency Response Plan Implementation Procedures requires that 
    certain actions be taken, up to and including shutdown of both 
    units, on the approach of a severe storm, such as a hurricane. The 
    probability of a loss of offsite power is maintained low by 
    prohibiting planned maintenance on two of the three 500 kV 
    transmission lines and associated relaying and devices within the 
    switchyard. Availability of the required offsite power sources will 
    be verified once per shift. In addition to the offsite power 
    sources, a temporary diesel generator will also be installed to 
    provide a backup onsite power source with the capacity to support 
    the safety-related loads of the shutdown unit.
        The boron dilution event and the fuel handling incident are the 
    only two accidents that are explicitly analyzed in the Updated Final 
    Safety Analysis Report for a shutdown unit. The potential accident 
    precursors such as core alterations, positive reactivity insertions, 
    movement of irradiated fuel and movement of heavy loads over 
    irradiated fuel, will be prohibited while No. 12 EDG is out-of-
    service for the temporary splice box installation. Therefore the 
    probability of a boron dilution event or fuel handling incident is 
    decreased during the operations allowed by this change. The 
    requirement to maintain containment penetration closure ensures that 
    the consequences of an accident would not be significantly 
    increased.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        A temporary diesel generator is being installed onto a 4 kV bus 
    of the shutdown unit while the dedicated EDG for this unit is 
    transferred to the operating unit for up to 14 days. This is an 
    extension of the same configuration allowed by Action Statements 
    3.8.1.2.b and 3.8.2.2.b with additional provision taken for the 
    Control Room Emergency Ventilation System (CREVS). The EDGs will be 
    aligned so that each train of the CREVS will have an emergency power 
    supply available. The proposed change has been evaluated and it has 
    been determined that it does not impair any existing safety-related 
    equipment needed to maintain the unit in a safe shutdown condition, 
    and does not create any new accident initiators. The operation of 
    the temporary diesel generator is familiar to the operators and is 
    not significantly different from typical operator activities.
        Therefore, the proposed change does not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The safety function provided by the AC electrical power sources 
    and associated distribution systems for a shutdown unit is to ensure 
    that the unit can be maintained in a safe shutdown condition, and 
    there is sufficient instrumentation and control capability available 
    for monitoring and maintaining the unit status. The proposed change 
    would allow the shutdown unit to be without a dedicated Class 1E 
    emergency power source for up to 14 days. This is an extension of 
    the outage time of seven days allowed by the Technical 
    Specifications for performing maintenance and inspections on No. 12 
    EDG. This proposed change will have no impact on the offsite power 
    sources.
        Several compensatory measures will be taken during this period 
    to ensure that a power source will be available for the shutdown 
    unit. These measures include requiring that two offsite power 
    sources are available, and a temporary diesel generator will be 
    installed capable of supplying the loads necessary to maintain the 
    unit in a safe condition. In addition, Technical Specifications 
    require several compensatory measures to reduce the potential for a 
    fuel handling incident and a boron dilution event. These measures 
    include prohibiting positive reactivity changes, suspending core 
    alterations, movement of irradiated fuel, and the movement of heavy 
    loads over irradiated fuel. Establishing containment penetration 
    closure further ensures that adequate margin of safety is 
    maintained. In addition, reduced inventory conditions of the Reactor 
    Coolant System will be prohibited during the 14-day period.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        In relation to the requested changes in the Unit 1 TSs:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The Control Room Emergency Ventilation System (CREVS) is 
    designed so that the Control Room can be occupied under all plant 
    conditions. The CREVS is required to maintain the Control Room 
    temperature and to filter the Control Room air in the event of a 
    radioactive release. When No. 21 Emergency Diesel Generator (EDG) is 
    being upgraded, No. 12 CREVS will be without a Class 1E emergency 
    power source. The CREVS is not an initiator in any previously 
    evaluated accidents. Therefore, the proposed change does not involve 
    an increase in the probability of an accident previously evaluated.
        The CREVS is required to maintain the Control Room habitable 
    following a radioactive release from a loss of coolant accident, a 
    main steam break, or a steam generator tube rupture. There is a very 
    low probability of an event occurring requiring Control Room 
    isolation during the 30-day period that it will take to upgrade No. 
    21 EDG. Requiring that the CREVS have both a normal power source and 
    an emergency power source available ensures that one train of the 
    system will be available so that the Control Room can be occupied 
    under these conditions. The probability of a loss of offsite power 
    is very low due to the highly redundant design of the offsite power 
    supply. Planned maintenance on three of the offsite power supplies 
    and associated relaying and devices within the switchyard will be 
    prohibited during the upgrade period to maintain the low probability 
    of a loss of offsite power event. Number 12 CREVS train will 
    continue to have its normal power source for all but approximately 
    four days when the bus will be de-energized to allow bus work that 
    is necessary to the tie-in of the Alternate AC diesel generator. 
    Number 11 CREVS will have both its normal and emergency power supply 
    available and this train is capable of maintaining the Control Room 
    habitable. In addition, a temporary diesel generator will be 
    installed to provide assurance that an emergency power source will 
    be available to No. 12 CREVS. The compensatory measures that will be 
    taken during this period will ensure that the proposed change does 
    not involve a significant increase in the consequences of an 
    accident previously evaluated.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The CREVS is not being modified by this proposed change. The 
    system will continue to operate in the same manner. Number 21 EDG 
    will operate in a similar manner after the upgrade and will be able 
    to support unit operation after all the testing is completed. The 
    installation of the temporary diesel generator during the upgrade 
    period has been evaluated to ensure that it does not create any new 
    accident initiators.
        Therefore, the proposed change does not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The operability of the CREVS during Modes 1 through 4 ensures 
    that the Control Room will remain habitable under all plant 
    conditions. The proposed change does not affect the function of the 
    CREVS. The proposed change will allow one train of the CREVS to be 
    without a Class 1E emergency power supply for up to 30 days. This 
    train will have the normal power supply available for all but 
    approximately four days to allow necessary bus work. The other train 
    of the CREVS will have both its normal and emergency power supplies 
    during this period. Compensatory measures that will be taken include 
    prohibiting planned maintenance on the required offsite power 
    sources and installing a temporary diesel generator of sufficient 
    capacity as a backup to the affected train. These measures will 
    maintain the current margin of safety. The upgrade to the existing 
    EDGs will provide additional margin for the electrical loading of 4 
    kV safety-related busses. The completion of the No. 21 EDG upgrade 
    will improve the margin of safety for the onsite electrical 
    distribution system.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: September 6, 1994
        Description of amendment request: The proposed amendment changes 
    the Pilgrim Nuclear Power Station Technical Specifications Sections 
    3.7.B.1.a, 3.7.B.1.c, 3.7.B.1.e, 3.7.B.2.a, and 3.7.B.2.c. The proposed 
    changes also add new sections 3.7.B.1.f and 3.7.B.2.e. These sections 
    require both trains of the Standby Gas Treatment (SGTS) and Control 
    Room High Efficiency Air Filtration (CRHEAF) System to be operable for 
    the initiation of fuel movement and during fuel handling operations 
    involving irradiated fuel.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Technical Specifications 3.7.B.1 and 3.7.B.2.e restrict the 
    movement of irradiated fuel when only one train of SGTS or one train 
    of CRHEAF are operable. Irradiated fuel movement may not begin and 
    may only continue for seven days when the Limiting Condition of 
    Operation is entered.
        Removing these restrictions during refueling operations does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated because compensatory measures will 
    be in place.
        When sections 3.7.B.1.f and 3.7.B.2.e are invoked fuel movement 
    will not commence until 5 days following plant shutdown and reactor 
    vessel will be flooded-up to elevation 114''. The 5 day period 
    provides decay-time before irradiated fuel movement begins. 
    Flooding-up elevation 114'' provides an enlarged inventory reducing 
    the possibility of a loss-of-coolant event exposing fuel such that 
    radioactive gasses are produced, an event SGTS and CRHEAF are 
    designed to mitigate.
        Other compensatory measures include requiring the SBO [station 
    blackout] diesel or the shutdown transformer to be operable prior to 
    and during the fuel movement. This adds defense-in-depth by making 
    available another power supply to the in-service safety-related bus. 
    Also, the substitution of a non-safety power supply to the SGTS and 
    CRHEAF ``inoperable'' systems while their safety-grade bus is out-
    of-service for maintenance will provide offsite power to the 
    ``inoperable'' train. While this electrical supply is not safety-
    grade, it is reliable and capable of powering the SGTS and CRHEAF 
    systems. The components of the ``inoperable'' trains will be 
    available with power from an alternate power source. The 
    compensatory connection to the non-safety grade bus gives added 
    confidence these trains can perform the design function although 
    they are not ``operable'' as defined by Technical Specifications.
        Operating Pilgrim in accordance with this proposed change does 
    not involve a significant increase in the probability or consequence 
    of an accident previously analyzed because compensatory measures 
    will be in force to: restrict the commencement of irradiated fuel 
    handling or new fuel handling over the spent fuel or core until 5 
    days following reactor shutdown; provide a reliable source of power 
    to the ``inoperable'' SGTS and CRHEAF systems; provide an enlarged 
    coolant inventory to protect irradiated fuel from the effects of an 
    inadvertent draindown of the vessel; and provide an additional 
    source of emergency power to the active SGTS and CRHEAF systems by 
    ensuring the operability of the SBO diesel generator or the Shutdown 
    Transformer.
        2. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Planned maintenance activities require removing a safety-related 
    bus and emergency diesel generator powering a train of SGTS and 
    CRHEAF from service. The redundant trains are not affected. The 
    affected trains of SGTS and CRHEAF will be connected to a non-safety 
    bus, allowing them to operate but not allowing them to be considered 
    operable under the purview of Technical Specifications. The proposed 
    change allows refueling activities to commence with one train of 
    SGTS and CRHEAF fully operable and the other train available but not 
    powered by its safety grade bus and associated emergency diesel 
    generator. Compensatory measures will be in effect during refueling 
    activities involving this configuration. The proposed changes do not 
    create the possibility of a new or different kind of accident from 
    the fuel-drop accident previously analyzed. Therefore, operating 
    Pilgrim in accordance with this change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously analyzed.
        3. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant reduction in the 
    margin of safety.
        SGTS and CRHEAF contribute to the margin of safety during fuel 
    handling by mitigating the consequences of a fuel-handling event. 
    Allowing an exception to the requirement of both trains of SGTS and 
    CRHEAF operable prior to or during fuel movement activities does not 
    involve a significant reduction in the margin of safety because the 
    first line of defense, the other SGTS and CRHEAF trains, will be 
    operable. The redundant trains will also be powered and operable in 
    all ways except the ``operable'' concept required by Technical 
    Specification.
        Hence, the actual condition of the equipment allows it to meet 
    its design function except under the strict Technical Specification 
    interpretation of operable, and the described compensatory measures 
    that will be in effect when the exception is employed, constrain the 
    potential impact on the margin of safety caused by using the 
    exception; therefore, operating Pilgrim in accordance with this 
    proposed Technical Specification request does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Walter R. Butler
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: September 6, 1994
        Description of amendment request: The proposed amendment would 
    reduce the Reactor Pressure Setpoint at which the shutdown cooling 
    system automatically isolates. This setpoint also isolates the low 
    pressure coolant injection valves when the shutdown cooling system is 
    in operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Technical Specification Table 3.2.A lists the instrumentation 
    that initiates primary containment isolation and also lists the trip 
    level setting (setpoints) for that instrumentation. The setpoint for 
    reactor high pressure is presently [less than or equal to] 110 psig 
    which was selected to provide protection for the RHR [residual heat 
    removal] low pressure suction piping against possible 
    overpressurization. This signal initiates a group 3 containment 
    isolation by closing the shutdown cooling isolation valves and the 
    Low Pressure Coolant Injection (LPCI) valves. To provide an optimal 
    solution to address Generic Letter 89-10, the motor-operated valves 
    which effect the isolation of the RHR suction piping (MO1001-47 and 
    MO1001-50) are being modified based on a lower differential pressure 
    in the design calculations. The setpoint is being reduced to ensure 
    plant operation is maintained in accordance with the new design and 
    to continue to provide the protection necessary against 
    overpressurization. This does not involve an increase in the 
    probability or consequences of an accident previously analyzed 
    because reducing the setpoint to less than what the technical 
    specifications currently requires is a change in the conservative 
    direction relative to protection of the piping. The LPCI injection 
    valves are designed for higher pressures and the proposed setpoint 
    change does not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        Technical Specification Table 3.2.B lists instrumentation that 
    initiates or controls the core and containment cooling systems and 
    also lists the trip level settings (setpoints) for that 
    instrumentation. The setpoint for reactor low pressure [less than or 
    equal to] 110 psig, is a permissive for the group 3 isolation of the 
    RHR inboard injection valves. Reducing the setpoint to [less than or 
    equal to] 76 psig is consistent with the design of the other group 3 
    isolation valves that receive the same signal and accomplishes the 
    isolation of the shutdown cooling system when there is a system 
    breach. Thus, revising this setpoint does not increase the 
    probability or consequences of an accident previously evaluated.
        2. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed setpoint change supports modifications made to the 
    shutdown cooling isolation valves to provide additional margin to 
    address Generic Letter 89-10 concerns. Reducing the setpoint for 
    this function continues to provide protection of the RHR suction 
    piping and ensures closure of the isolation valves. Therefore, 
    revising the reactor high pressure setpoint to [less than or equal 
    to] 76 psig for instrumentation that initiates primary containment 
    isolation (Table 3.2.A) does not create the possibility of a new or 
    different kind of accident previously evaluated. Similarly, the 
    revision of the reactor low pressure setpoint to [less than or equal 
    to] 76 psig for instrumentation that initiates or controls the core 
    and containment cooling systems does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant reduction in a 
    margin of safety.
        The purpose of the setpoint for reactor pressure in Table 3.2.A 
    and 3.2.B is to provide protection for the RHR suction piping and 
    ensure proper isolation for unlikely piping breaches. Changing the 
    setpoint to a lower value is consistent with modifications being 
    made to the shutdown cooling isolation valves. The margin of safety 
    for this setpoint was established to protect the RHR suction piping 
    from overpressurization and to ensure that primary containment 
    integrity could be established by the isolation valves on a Group 3 
    isolation. A margin of safety for protecting the RHR suction piping 
    exists due to the difference between the design pressure of the 
    piping and the setpoint specified in the technical specifications. 
    Reducing the setpoint increases the difference between the design 
    pressure of the piping and the setpoint hence, this margin of safety 
    is increased. The margin of safety established for primary 
    containment isolation valves is maintained by specifying a setpoint 
    which corresponds to the closing differential pressure of the valves 
    under postulated accident conditions. The setpoint change does not 
    reduce the design margins established to ensure the valves perform 
    their design isolation function when required. The low pressure 
    coolant injection valves that receive this same signal are designed 
    for higher pressures than the current setpoint of [less than or 
    equal to] 110 psig and, therefore, a lower setpoint increases the 
    margin of safety. Thus, the proposed amendment does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Walter R. Butler
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: September 6, 1994
        Description of amendment request: The proposed amendment would 
    remove Technical Specification section 4.5.H.4, a section which 
    requires the testing and calibration of pressure switches in certain 
    emergency core cooling system (ECCS) lines.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The Operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    [***].
        The discharge piping for ECC systems is maintained filled to 
    prevent water hammer during automatic pump starts. Monthly venting 
    is the primary means of ensuring filled discharge piping. The 
    pressure switches are an adjunct to such venting. Hence, piping in 
    the Core Spray System, the Low Pressure Coolant Injection System 
    (LPCI), the High Pressure Coolant Injection (HPCI) system, and the 
    Reactor Core Isolation Coolant (RCIC) system are all equipped with 
    pressure switches that detect pressure decay in the discharge piping 
    of these systems.
        This proposed change does not change Pilgrim's configuration or 
    equipment. The switches perform a surveillance function and do not 
    provide a signal needed to prevent or mitigate an accident. The 
    switches will continue to perform their surveillance function and 
    their surveillance and calibration will be performed in accordance 
    with Pilgrim procedures. Removal of section 4.5.H.4 eliminates the 
    possibility of inoperable switches forcing the shutdown of Pilgrim 
    or the alternative of declaring an operable safety system inoperable 
    because of its association with these switches.
        Technical Specifications will continue to require venting the 
    discharge piping high point when the systems are configured such 
    that water hammer can occur. (sections 4.5.H.1, 4.5.H.2 and 
    4.5.H.3). Thus, the application of this proposed change does not 
    reduce the Technical Specifications intent of reducing the 
    likelihood of discharge piping water hammer. Therefore, operating 
    Pilgrim Station in accordance with the proposed amendment will not 
    involve a significant increase in the probability or consequences of 
    an accident previously analyzed.
        2. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Section 4.5.H's purpose is to maintain the ECCS discharge piping 
    filled to prevent water hammer. The purpose of the pressure switches 
    is to detect voids in ECCS discharge piping to prevent the 
    possibility of damage due to water hammer. These switches are not 
    safety-related, have no automatic functions, and are not relied on 
    to prevent or mitigate an accident. Instead, they enhance the 
    existing discharge pipe venting surveillance requirements by 
    detecting void formation in discharge pipe.
        The switches will continue to perform their surveillance 
    function through Pilgrim procedures. Venting will continue to be 
    required by Technical Specifications. Therefore, operating Pilgrim 
    in accordance with this proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated because the proposed change does not impair the 
    detection of conditions necessary to produce a water hammer in the 
    discharge piping.
        3. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant reduction in a 
    margin of safety.
        The discharge piping pressure switches are surveillance 
    instruments and act as a secondary means of protecting the discharge 
    piping from conditions that can produce water hammer. They are not 
    relied on to prevent or mitigate accidents. Hence, these switches do 
    not significantly impact safety because they are not the primary 
    means of preventing discharge piping water hammer. Therefore, 
    removing the pressure switches from Technical Specifications 
    potentially contributes to plant availability but does not involve a 
    significant reduction in a margin of safety because the primary 
    method of detection (venting) remains and the switches will continue 
    to be subject to procedural controls.
        This proposed change has been reviewed and recommended for 
    approval by the Operations Review Committee and reviewed by the 
    Nuclear Safety Review and Audit Committee.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Walter R. Butler
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: September 6, 1994
        Description of amendment request: The proposed amendment would 
    relocate the alarms for the drywell to suppression chamber vacuum 
    breakers to a different annunciator panel.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously identified.
        The proposed change relocates annunciators in the control room 
    but does not change their designed function or setpoint.
        The Annunciator System is non-safety related and performs no 
    direct safety function. No accident initiators are being affected by 
    this proposed change. Accident mitigating systems remain operable, 
    and accident scenarios are unaffected.
        2. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously analyzed.
        Relocating the Drywell to Suppression Chamber annunciator from 
    one control room panel to another does not create the possibility of 
    a new or different kind of accident. This modification does not 
    modify the setpoints or functions of the annunciators. Hence, it is 
    administrative and proposed to allow relocation which is currently 
    constrained by the current Technical Specifications level of detail.
        3. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant reduction in the 
    margin of safety.
        The equipment being relocated is non-safety related and its 
    relocation does not impact the margin of safety. This relocation is 
    proposed to enhance the operator's ability to identify and analyze 
    abnormal events.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Walter R. Butler
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois;Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: June 13, 1994, as supplemented on 
    October 7, 1994.
        Description of amendment request: The proposed amendment would make 
    several changes to the Administrative Controls in Section 6 of 
    Technical Specifications (TS) for Byron and Braidwood stations. The 
    proposed changes include: (1) a change to the submittal frequency of 
    the Radiological Effluent Release Report, (2) a revision to the Shift 
    Technical Advisor description, (3) clarification of the Shift 
    Engineer's responsibilities, and (4) editorial changes. The references 
    to the Semiannual Radiological Effluent Release Report are also revised 
    in other sections of the TS. The proposed change in the October 7, 
    1994, submittal revised TS 6.3.1 to include generic descriptions of 
    personnel who fulfill the responsibilities of a radiation protection 
    manager. This supplements the information that was published in the 
    Federal Register on August 3, 1994 (59 FR 39581).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes to Section 6 of Technical Specifications do 
    not affect any accident initiators or precursors and do not change 
    or alter the design assumptions for the systems or components used 
    to mitigate the consequences of an accident.
        The proposed changes are administrative in nature and provide 
    clarification. These changes provide consistency with station 
    procedures, programs, the Code of Federal Regulations, other 
    Technical Specifications, and Standard Technical Specifications. 
    These changes do not impact any accident previously evaluated in the 
    Updated Final Safety Analysis Report.
        B. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not affect the design or operation of 
    any system, structure, or component in the plant. There are no 
    changes to parameters governing plant operation; no new or different 
    type of equipment will be installed. The proposed changes are 
    considered to be administrative changes. All responsibilities 
    described in Technical Specifications for management activities will 
    continue to be performed by qualified individuals.
        C. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect the margin of safety for any 
    Technical Specification. The initial conditions and methodologies 
    used in the accident analyses remain unchanged, therefore, accident 
    analysis results are not impacted.
        The proposed changes are administrative in nature and have no 
    impact on the margin of safety of any Technical Specification. They 
    do not affect any plant safety parameters or setpoints. The 
    descriptions for the Shift Technical Advisor and Shift Engineer are 
    clarified, however, include no reduction to their responsibilities.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: Robert A. Capra
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of amendment request: September 13, 1994
    
        Description of amendment request: The amendments replace 
    Containment Systems technical specification (TS) 3.6.2.2, ``Spray 
    Additive System'' with a new Emergency Core Cooling Systems TS 3.5.5, 
    ``ECCS Recirculation Fluid pH Control System.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The proposed change involves replacement of concentrated 
    NaOH injected via the containment spray system with trisodium 
    phosphate (TSP) stored in the containment and dissolved in the sump 
    recirculation solution to maintain acceptable post accident spray/
    recirculation solution chemistry. Deletion of the concentrated NaOH 
    will eliminate a personnel hazard. The pH control system functions 
    in response to an accident and does not involve or have any effect 
    on any initiating event for any accident previously evaluated. 
    Operation under the proposed amendment will continue to ensure that 
    iodine potentially released post-LOCA is retained in the sump 
    solution, and resultant offsite and control room thyroid doses are 
    within the limits of 10 CFR 100 and 10 CFR 50, Appendix A, General 
    Design Criterion 19, respectively.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The deleted equipment is isolated from the remaining 
    equipment by blind flanges, locked closed valves, cut and capped 
    piping, determinated and/or spared cables; and interfaces are 
    analyzed to ensure the remaining required equipment meets applicable 
    original design requirements. The new equipment (TSP and baskets) is 
    a passive pH control system and is supported and analyzed to ensure 
    there are no adverse interfaces (e.g. pipe break, jet impingement, 
    seismic) with existing equipment, systems, or structures.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety. The slight change in recirculation solution 
    pH maintains adequate protection against chloride induced stress 
    corrosion cracking of austenitic stainless steel and maintains the 
    capability of the solution to retain iodine. It results in an 
    insignificant increase in the post-accident rate of hydrogen 
    generation, which remains well within the existing capacity of the 
    hydrogen recombiners. The increased mass in the containment will 
    have no significant impact on post-accident flood levels, 
    recirculation solution boron concentration, or peak clad 
    temperatures. No other operating parameters for systems, structures, 
    or components assumed to operate in the safety analysis are changed. 
    The offsite and control room doses meet the limits of 10 CFR 100 and 
    GDC 19 respectively. Because the trisodium phosphate is nonvolatile 
    and the baskets are protected with solid covers and are located 
    slightly above the floor in the containment where access is strictly 
    controlled, a surveillance interval of once per refueling outage 
    provides assurance that the TSP will be available when required.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308
        NRC Project Director: Herbert N. Berkow
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: September 26, 1994
        Description of amendment request: The proposed license amendment 
    would revise the ``Plan for the Long Range Planning Program'' by 
    changing the semi-annual reporting period to annual, and to reflect 
    refined evaluation criteria and assessment methodology; and, to 
    incorporate the necessary changes to the license condition wording.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or consequences of an accident previously 
    evaluated. The proposed revision to the Facility Operating License 
    does not affect the safety analysis and does not involve any 
    physical changes to the plant, nor any changes in the format or 
    restraints on plant operations, and only contemplates a change to 
    the Plan for the Long Range Planning Program currently approved by 
    the NRC in license condition 2.C.(6). Therefore, this change will 
    not increase the probability of previously analyzed accidents 
    because it involves no direct plant modification or change in 
    operation, and hence, it is also unrelated to the possibility of 
    increasing the consequences of previously analyzed accidents.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any previously evaluated. The proposed 
    revision to the Facility Operating License does not affect the 
    safety analysis and does not involve any physical changes to the 
    plant, nor any changes in the format or restraints on plant 
    operations, and only contemplates a change to the Plan for the Long 
    Range Planning Program currently approved by the NRC in license 
    condition 2.C.(6). Therefore, this change has no effect on the 
    possibility of creating a new or different kind of accident from any 
    previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety. The proposed revision to the Facility Operating License does 
    not involve any physical changes to the plant, nor any changes in 
    the format or restraints on plant operations, and only contemplates 
    a change to the Plan for the Long Range Planning Program currently 
    approved by the NRC, in license condition 2.C.(6). Therefore, the 
    overall margin of safety for the plant is maintained.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Phillip F. McKee
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: September 26, 1994
        Description of amendment request: The proposed license amendment 
    would revise the ``Plan for the Long Range Planning Program'' by 
    changing the semi-annual reporting period to annual, and to reflect 
    refined evaluation criteria and assessment methodology; and, to 
    incorporate the necessary changes to the license condition wording.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or consequences of an accident previously 
    evaluated. The proposed revision to the Facility Operating License 
    does not affect the safety analysis and does not involve any 
    physical changes to the plant, nor any changes in the format or 
    restraints on plant operations, and only contemplates a change to 
    the Plan for the Long Range Planning Program currently approved by 
    the NRC in license condition 2.C.(9). Therefore, this change will 
    not increase the probability of previously analyzed accidents 
    because it involves no direct plant modification or change in 
    operation, and hence, it is also unrelated to the possibility of 
    increasing the consequences of previously analyzed accidents.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any previously evaluated. The proposed 
    revision to the Facility Operating License does not affect the 
    safety analysis and does not involve any physical changes to the 
    plant, nor any changes in the format or restraints on plant 
    operations, and only contemplates a change to the Plan for the Long 
    Range Planning Program currently approved by the NRC in license 
    condition 2.C.(9). Therefore, this change has no effect on the 
    possibility of creating a new or different kind of accident from any 
    previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety. The proposed revision to the Facility Operating License does 
    not involve any physical changes to the plant, nor any changes in 
    the format or restraints on plant operations, and only contemplates 
    a change to the Plan for the Long Range Planning Program currently 
    approved by the NRC, in license condition 2.C.(9). Therefore, the 
    overall margin of safety for the plant is maintained.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Phillip F. McKee
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: September 26, 1994
        Description of amendment request: The proposed amendment would 
    revise the Cooper Nuclear Station (CNS) Technical Specifications, 
    Section 3.5.C ``HPCI System,'' to increase the minimum pressure at 
    which the High Pressure Coolant Injection (HPCI) System is required to 
    be OPERABLE from greater than 113 psig to greater than 150 psig.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Evaluation
        The change in the reactor vessel pressure at which the High 
    Pressure Coolant Injection (HPCI) System must be operable from
        113 psig to 150 psig will not result in a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The HPCI System is designed to provide adequate reactor 
    vessel coolant injection for small break accidents where the reactor 
    vessel remains pressurized. Therefore, the HPCI System provides a 
    means of responding to previously analyzed accidents. Changing the 
    lower bound reactor vessel pressure limit at which the HPCI System 
    must be operable does not affect any of the accident initiation 
    sequences previously analyzed, and therefore this proposed change 
    will not result in an increase in the probability of any accident 
    previously analyzed.
        The change in the required pressure at which the HPCI System 
    must be operable from 113 psig to 150 psig will not involve a 
    significant increase in the consequences of any accident previously 
    evaluated. Increasing this minimum pressure at which the HPCI System 
    must be OPERABLE will not affect the availability of other systems 
    which provide standby core cooling. The CNS Core Standby Cooling 
    Systems (CSCS), which consist of the HPCI System, the Automatic 
    Depressurization System (ADS), the Low Pressure Coolant Injection 
    (LPCI) System, and the Core Spray (CS) System, are designed to cover 
    the spectrum of loss-of-coolant accidents. For large break events, 
    the reactor vessel will depressurize below the point where the HPCI 
    System is OPERABLE, and single failure proof core cooling is 
    provided by a combination of the LPCI and CS systems. For small 
    break events wherein the reactor vessel does not rapidly 
    depressurize, the HPCI System is designed to provide core cooling 
    with a reactor vessel pressure range of 1120 psig to 150 psig. Upon 
    failure of the HPCI System to provide adequate core cooling, the ADS 
    in conjunction with the LPCI and CS systems provide single failure 
    proof assurance of adequate core cooling. The Low Pressure Systems 
    (LPCI and CS) are designed and required to provide core cooling at 
    reactor pressures below 150 psig.
        The District performed calculations which have determined that 
    the low pressure Core Standby Cooling systems are capable of 
    providing adequate core cooling with a reactor pressure of 150 psig 
    under the most degraded pump conditions, i.e., pump performance at 
    minimum Technical Specifications requirements. Additionally, the 
    District reviewed applicable engineering calculations to ensure that 
    no calculations were relying on the HPCI System to provide degraded 
    flow to the reactor vessel during any accident scenario or 
    transient. Based on the diverse means of providing adequate core 
    cooling for the spectrum of loss-of-coolant accidents, and the 
    capability of the low pressure core cooling systems to provide 
    adequate core cooling at 150 psig and below, changing the required 
    pressure at which HPCI must be operable from 113 psig to 150 psig 
    will not change the capability to provide adequate core cooling 
    following postulated events.
        The proposed changes do not alter the conditions or assumptions 
    in any of the Updated Safety Analysis Report (USAR) accident 
    analyses. Since the USAR accident analyses remain bounding, the 
    radiological consequences previously evaluated are not adversely 
    affected by the proposed changes. Therefore, it can be concluded
        that the proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2.Does the proposed License Amendment create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated?
    
        Evaluation
        The proposed changes introduce no new failure modes for any 
    plant system or component important to safety nor has any new 
    limiting failure been identified as a result of the proposed 
    changes. Increasing the minimum reactor pressure at which the HPCI 
    System is required to be OPERABLE will not cause an unplanned 
    initiation of the HPCI System or any other plant system or 
    equipment, nor will the change impede the initiation of any required 
    safety system. The HPCI System relies on the containment suppression 
    pool, emergency condensate storage tanks, plant D.C. electrical 
    system, and the reactor low water level and high drywell pressure 
    instrumentation to adequately operate. The proposed increase in the 
    minimum reactor pressure at which the HPCI System would be required 
    OPERABLE will not affect the equipment of these systems, nor will 
    the change affect the physical configuration of the HPCI System. 
    There will be no change in the types or increase in the amount of 
    effluents released offsite. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Does the proposed change create a significant reduction in the 
    margin of safety?
        Evaluation
        Changing the reactor vessel pressure at which the HPCI System 
    must be OPERABLE from 113 psig to 150 psig will not constitute a 
    significant reduction in the margin of safety. As stated in the 
    Technical Specifications Bases Section 3.5.C, the HPCI System is 
    designed to provide rated cooling water flow for reactor pressures 
    ranging from 1120 psig to 150 psig. The HPCI is not designed to 
    provide rated cooling water flow at reactor pressures below 150 
    psig. At reactor operating pressures below 150 psig, the low 
    pressure core cooling systems are required to be available, are 
    capable of fulfilling their functions, and provide the required flow 
    in the low pressure regions below 150 psig. Additionally, the 
    combination of the ADS, LPCI and CS systems provide additional means 
    of providing adequate core cooling at any reactor pressure. 
    Therefore the proposed change to increase the minimum reactor 
    pressure at which the HPCI System is required to be operable to 
    greater than 150 psig will not significantly reduce the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Auburn Public Library, 118 
    15th Street, Auburn, Nebraska 68305
        Attorney for licensee: Mr. G.D. Watson, Nebraska Public Power 
    District, Post Office Box 499, Columbus, Nebraska 68602-0499
        NRC Project Director: William D. Beckner
    
    Northeast Nuclear Energy Company (NNECO), Docket No. 50-245, 
    Millstone Nuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of amendment request: September 9, 1994
        Description of amendment request: The proposed revision to the 
    Technical Specifications would delete the requirement for a special 
    test of the alternate train when one train is inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed changes in accordance with 
    10CFR50.92 and concludes that the changes do not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    compromised. The proposed changes do not involve an SHC because the 
    changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed changes do not affect the operation of the APR 
    [automatic pressure relief] or FWCI [feedwater coolant injection] 
    subsystems, nor the SBGT [standby gas treatment] system. The 
    proposed changes do not modify the required actions described in the 
    LCOs [limiting conditions for operation] when either one or both 
    circuits of SBGT or an APR valve are determined to be inoperable. 
    The proposed changes will increase the availability of the APR 
    subsystem by eliminating a surveillance requirement that causes the 
    actuation logic to be taken out of service for testing when one 
    valve is determined to be inoperable. The proposed changes will not 
    affect the availability of the remaining circuit of SBGT since 
    testing does not remove the train from service.
        Both the SBGT and APR systems function to mitigate the 
    consequences of postulated accidents. As such, modification to the 
    surveillance requirements does not create a significant increase in 
    the probability of an accident. Eliminating the alternate train 
    testing requirement will not significantly increase the consequences 
    of a postulated accident. The added assurance that the APR actuation 
    logic is operable which is provided by Section 4.5.D.2 is not 
    sufficient to justify the loss of safety function during testing, or 
    the increased risk of inadvertent operation of the APR valves or the 
    FWCI subsystem. While Technical Specification 4.7.B.3.c does not 
    remove the remaining SBGT circuit from service, reasonable assurance 
    of operability is provided by Technical Specification 4.7.B.2.d 
    which requires a monthly demonstration of operability of each train 
    of the SBGT system.
        Therefore, no significant increase in the probability or 
    consequences of an accident previously analyzed would occur.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes delete the requirement to demonstrate the 
    operability of the remaining APR valves actuation logic, the FWCI 
    subsystem, and the alternate circuit of SBGT immediately and daily 
    thereafter when one APR valve or one circuit of SBGT is determined 
    to be inoperable. The proposed changes do not add or change any 
    equipment or logic. The proposed changes also do not alter any 
    system operability requirements. These changes only affect the 
    number of surveillance tests which must be performed. They do not 
    affect the test methodology for any of these systems.
        Since there are no changes to the function, operation, or 
    surveillance test methodology of any of these systems, the 
    possibility of a new or different kind of accident is not created.
        3. Involve a significant reduction in the margin of safety.
        The proposed changes delete the requirement to demonstrate the 
    operability of the remaining APR valves actuation logic, the FWCI 
    subsystem, and the alternate circuit of SBGT immediately and
        daily thereafter when one APR valve or one circuit of SBGT is 
    determined to be inoperable. The elimination of the additional 
    assurance that the actuation logic for the remaining APR valves and 
    the FWCI subsystem is operable is more than offset by the increase 
    in the margin of safety which is created by eliminating a 
    requirement to remove the safety system from service for testing. 
    The margin of safety for the SBGT system is not significantly 
    reduced since this system is tested monthly in accordance with 
    Technical Specification 4.7.B.2.d.
        Assurance of operability is provided by the normal, scheduled 
    surveillances which have been established at a sufficient interval 
    to provide reasonable assurance of operability. Therefore, the 
    proposed changes do not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    DiabloCanyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: September 20, 1994 (Reference LAR 94-
    08)
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant Unit Nos. 1 and 2 to revise surveillance requirements (SRs) 
    as recommended by NRC Generic Letter (GL) 93-05, ``Line-Item Technical 
    Specification Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operation.'' The specific TS changes proposed are 
    as follows:
        (1) TS SR 4.1.3.1.2 would be revised to change the frequency for 
    testing the movability of the control rods from at least once per 31 
    days to at least once per 92 days.
        (2) TS 3/4.3.2, Table 4.3-2, ``Engineered Safety Features Actuation 
    System Instrumentation Surveillance Requirements,'' Functional Unit 
    3.c.4), and TS 3/4.3.3.1, Table 4.3-3, ``Radiation Monitoring 
    Instrumentation for Plant Operations SRs,'' would be revised to change 
    the monthly channel functional test to a quarterly channel functional 
    test.
        (3) The proposed changes to TS 3/4.5.1 are as follows: (a)
        TS SR 4.5.1.1a.1) would be revised to more clearly state that the 
    accumulator water volume and pressure must be verified to be within 
    their limits. (b) TS SR 4.5.1.1b. would be revised to specify that the 
    boron concentration surveillance is not required to be performed if the 
    accumulator makeup source was the refueling water storage tank (RWST). 
    (c) TS SR 4.5.1.2 would be relocated to plant procedures.
        (4) TS SR 4.5.2c.2) would be revised to clarify that a separate 
    containment entry to verify the absence of loose debris is not required 
    after each containment entry.
        (5) TS SR 4.6.2.1d. would be revised to change the frequency for a 
    containment spray header flow test from at least once per 5 years to at 
    least once per 10 years.
        (6) TS SR 4.6.4.2a. would be revised to change the verification of 
    the minimum hydrogen recombiner sheath temperature from at least once 
    per 6 months to at least once each refueling interval.
        (7) TS SR 4.7.1.2.1 would be revised to change the surveillance 
    frequency for testing each auxiliary feedwater (AFW) pump from at least 
    once per 31 days to at least once per 92 days on a staggered test 
    basis.
        (8) TS SR 4.10.1.2 would be revised to lengthen the allowed period 
    of time for a rod drop test from 24 hours to 7 days prior to reducing 
    shutdown margin to less than the limits of TS 3.1.1.1.
        (9) TS SR 4.11.2.6 would be revised to change the surveillance 
    frequency from 24 hours to 7 days when radioactive material is being 
    added to the gas decay tanks and to add a requirement to monitor 
    radioactive material concentrations in the gas decay tanks at least 
    once per 24 hours when system degassing operations are in progress.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The changes proposed in this LAR [license amendment request] are 
    consistent with the guidance provided in GL 93-05. The proposed 
    changes eliminate testing that is likely to cause transients or 
    excessive wear of equipment. An evaluation of these changes 
    indicates that they result in a net benefit to plant safety. The 
    evaluation considered:
        (i) Unavailability of safety equipment due to testing
        (ii) Initiation of significant transients due to testing
        (iii) Actuation of engineered safety features that unnecessarily 
    cycle safety equipment
        (iv) Importance to safety of that system or component
        (v) Failure rate of that system or component
        (vi) Effectiveness of the test in discovering the failure
        As a result of the decrease in the testing frequencies, the risk 
    of testing causing a transient and equipment degradation will be 
    decreased, and the reliability of the equipment will not be 
    significantly decreased.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not affect the method of operating any 
    equipment at DCPP. Additionally, the proposed changes do not result 
    in a physical modification to any plant equipment.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes affect the surveillance requirements. There 
    is no decrease in equipment reliability by the elimination of 
    unnecessary testing that increases the risk of transients or 
    equipment degradation.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Theodore R. Quay
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: September 19, 1994
        Description of amendment request: The proposed license amendment 
    would revise Technical Specification (TS) 3/4.7.4, ``Snubbers,'' and 
    its bases, in accordance with NRC Generic Letter (GL) 90-09, 
    ``Alternative Requirements for Snubber Visual Inspection Intervals and 
    Corrective Actions.'' One difference from GL 90-09 is that the initial 
    inspection interval using the new criteria would be 18 months from the 
    conclusion of the visual inspection conducted during the recently 
    completed refueling outage. Additional changes to the TS would be made 
    to ensure consistency with the revised snubber visual inspection 
    interval schedule.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change has been reviewed for PNPP and has been 
    determined not to involve a significant hazards consideration based 
    on the following:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Implementing the guidance recommended in a GL 90-09 will not 
    introduce any new failure mode and will not alter any assumptions 
    previously made in evaluating the consequences of an accident. As 
    stated in the GL, the proposed alternate schedule for visual 
    inspections of snubbers will maintain the same operability 
    confidence level as the existing schedule. Also, the surveillance 
    requirements and schedule for snubbers functional testing remains 
    the same, providing a 95 percent confidence level that 90 percent to 
    100 percent of the snubbers operate within the specified acceptance 
    limits. The proposed visual inspection schedule is separate from the 
    functional testing and provides additional confidence that the 
    installed snubbers will serve their design function and are being 
    maintained operable. The proposed change does not affect limiting 
    safety system settings or operating parameters, and does not modify 
    or add any accident initiating events or parameters. No hardware 
    modifications are associated with these changes. Therefore, the 
    proposed change does not significantly increase the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Implementing the recommendations provided in GL 90-09 does not 
    involve any physical alterations to plant equipment, changes to 
    setpoints or operating parameters, nor does it involve any accident 
    initiating event. As stated in the GL, the alternate schedule for 
    snubber visual inspections maintains the same confidence level as 
    the existing schedule. In addition to the visual inspections, 
    functional testing of snubbers, which provides a 95 percent 
    confidence level that 90 percent to 100 percent of the snubbers 
    operate within specified acceptance limits, will continue to be 
    performed. Since this TS change does not physically alter the plant 
    equipment and the snubber confidence level remains the same there 
    will not be any new or different accident resulting from snubber 
    failure from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change incorporates surveillance requirements for 
    snubber visual inspection intervals that are consistent with the 
    guidance provided in GL 90-09. As stated in the GL, the proposed 
    snubber visual inspection interval maintains the same confidence 
    level as the existing snubber visual inspection interval. This 
    surveillance requirement does not alter the current Limiting 
    Condition for Operation or the accompanying actions for the 
    snubber(s). The requirement for functional testing of safety-related 
    snubbers is unchanged and remains the basis for the established 
    margin of safety and assures a 95 percent confidence level that 90 
    percent to 100 percent of the snubbers operate within the specified 
    acceptance limits. The functional testing along with the proposed 
    visual inspection provides adequate assurance that the snubber will 
    perform its intended function. Therefore, the proposed change does 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037NRC Acting Project 
    Director: Cynthia A. Carpenter
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendment request: September 12, 1994
        Description of amendment request: The proposed amendment would 
    modify Point Beach Nuclear Plant Technical Specification (TS) 15.3.3, 
    ``Emergency Core Cooling System, Auxiliary Cooling Systems, Air 
    Recirculation Fan Coolers, and Containment Spray,'' by incorporating 
    allowed outage times similar to those contained in NUREG 1431, Revision 
    0, ``Westinghouse Owner's Group Improved Standard Technical 
    Specifications,'' and by clarifying the operability requirements for 
    the service water pumps. The proposed changes would also clarify the 
    completion times for placing a unit in hot or cold shutdown if a 
    limiting condition for operation cannot be met.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        In accordance with the requirements of 10 CFR 50.91(a), 
    Wisconsin Electric Power Company (Licensee) has evaluated the 
    proposed changes against the standards of 10 CFR 50.92 and has 
    determined that the operation of Point Beach Nuclear Plant, Units 1 
    and 2, in accordance with the proposed amendments, does not present 
    a significant hazards consideration.
        A proposed facility operating license amendment does not present 
    a significant hazards consideration if operation of the facility in 
    accordance with the proposed amendment will not:
        1. Create a significant increase in the probability or 
    consequences of an accident previously evaluated; or
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or
        3. Will not create a significant reduction in a margin of 
    safety.
        CRITERION 1
        Operation of this facility under the proposed Technical 
    Specifications change will not create a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    proposed changes to the allowed out of service times have no impact 
    on the probability of an accident occurring. This equipment being 
    out of service is not an initiator for any accident previously 
    evaluated. There is no physical change to the facility, its systems 
    or its operation.
        The clarification of service water pump operability requirements 
    will ensure redundant train capability to mitigate the consequences 
    of an accident which has been previously evaluated. Extending the 
    allowed out of service times for the safety injection, residual heat 
    removal, and containment spray pumps and valves and residual heat 
    removal heat exchangers does not create a significant increase in 
    the consequences of an accident previously evaluated. The proposed 
    changes are consistent with the Westinghouse Improved Standard 
    Technical Specifications, NUREG 1431, Revision 0. Plant specific 
    analysis demonstrates the proposed changes do not pose an undue risk 
    and thus will not result in a significant increase in the 
    consequences of an accident.
        CRITERION 2
        Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The safety injection, containment spray, and residual heat removal 
    pumps and valves and residual heat removal heat exchangers are used 
    to mitigate the consequences of an accident and are not normally in 
    use during power operation. The availability of these components 
    does not effect the possibility of a new or different type of 
    accident. The service water pumps are normally in use during power 
    operation. The proposed change will ensure that redundant train 
    capability exists. Minimum service water pump requirements remain 
    the same. The failure modes of the service water system remain 
    unchanged. Therefore, extending the allowed out of service time does 
    not create the possibility of a different type of accident than 
    previously evaluated.
        CRITERION 3
        Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety. The proposed Technical Specification changes 
    revise the allowed outage times for the safety injection, residual 
    heat removal, and containment spray pumps and valves and residual 
    heat removal heat exchangers to 72 hours. This change will allow 
    more time for corrective maintenance to be performed on these 
    components, if required, and avoid potential transients and 
    challenges to safety systems associated with a required shutdown of 
    the unit without the specific safety related equipment operable. The 
    proposed changes are consistent with the Westinghouse Improved 
    Standard Technical Specifications, NUREG 1431, Revision 0. Plant 
    specific analysis demonstrates the changes do not pose an undue risk 
    and thus will not result in a significant reduction in a margin of 
    safety. The clarification to the specification for service water 
    pump operability may increase the margin of safety by ensuring that 
    redundant train capability exists.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 15, 1994
        Description of amendment request: This amendment would revise 
    Technical Specification 3/4.3.3, Table 4.3-3, ``Radiation Monitoring 
    Instrumentation For Plant Operations Surveillance,'' to change the 
    analog channel operational test (ACOT) interval from monthly to 
    quarterly for the following radiation monitors: (1) Containment 
    Atmosphere - Gaseous Radioactivity - High (GT-RE-31 and 32); (2) 
    Gaseous Radioactive - RCS Leakage Detection (GT-RE-31 and 32); (3) 
    Particulate Radioactivity - RCS Leakage Detection (GT-RE-31 and 32); 
    (4) Fuel Building Exhaust - Gaseous Radioactivity - High (GG-RE-27 and 
    28); (5) Criticality - High Radiation Level (SD-RE-37 and 38; SD-RE-35 
    and 36); (6) Control Room Air Intake - Gaseous Radioactivity - High 
    (GK-RE-04 and 05).
        This proposed change is identified as a line-item improvement in 
    Section 5.14 of Generic Letter 93-05, ``Line-Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operations.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a Significant Increase in the Probability of 
    Consequences of an Accident Previously Evaluated
        The probability of occurrence and the consequences of an 
    accident evaluated previously in the Updated Safety Analysis Report 
    (USAR) are not increased due to the proposed technical specification 
    change. Review of past ACOT history for the affected monitors 
    revealed that these monitors have experienced no calibration or 
    setpoint-related problems since the beginning of plant operation. 
    Increasing the ACOT frequency for these monitors will not adversely 
    affect system operability, and this change would reduce the 
    potential for instrument damage, thus effectively increasing system 
    reliability and availability. These radiation monitors are not 
    accident-initiating equipment, so increasing the surveillance 
    interval on these monitors will not affect the probability of any 
    accident previously evaluated. In addition, for the monitors listed 
    in TS Table 4.3-3, no credit is taken in the plant accident analyses 
    in Chapter 15 of the USAR for any automatic actuation function 
    generated as a result of a radiation monitor signal. On these bases 
    it is concluded that the probability and consequences of the 
    accidents previously evaluated in the USAR are not increased.
        2. Create the Possibility of a New or Different Kind of Accident 
    from any Previously Evaluated
        No new type of accident or malfunction will be created since the 
    radiation monitors are not accident-initiating equipment. The 
    proposed change merely increases the ACOT interval for the affected 
    radiation monitors, and does not change the method and manner of 
    plant operation. The safety design bases in the USAR have not been 
    altered. Thus, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        3. Involve a Significant Reduction in the Margin of Safety
        The proposed changes do not change the plant configuration in a 
    way that introduces a new potential hazard to the plant and do not 
    involve a significant reduction in the margin of safety. The 
    proposed changes do not affect applicable safety analysis acceptance 
    criteria and will not affect system operating conditions. In 
    addition, plant operating experience has shown that these monitors 
    have not experienced calibration of setpoint-related failures since 
    the beginning of plant operation. Therefore, it is concluded that 
    the margin of safety, as described in the bases to any technical 
    specification, is not reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: Theodore R. Quay
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 22, 1994
        Description of amendment request: The proposed amendment revises 
    Technical Specification (TS) 6.2.2.g, 6.3.1.b, and 6.12.1.c to reflect 
    title changes in the Wolf Creek Nuclear Operating Corporation (WCNOC) 
    organization. The title Supervisor Operations in TS 6.2.2.g is being 
    changed to Superintendent Operations. The title Radiation Protection 
    Manager in TS 6.3.1.b and the title Manager Radiation Protection in TS 
    6.12.1.c are being changed to Superintendent Radiation Protection. The 
    title changes do not represent any changes in reporting relationships, 
    job responsibilities, or overall organizational changes. This request 
    supersedes a request for amendment dated April 19, 1994, which was 
    noticed on June 22, 1994 (59 FR 32239)
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Proposed changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    These changes involve administrative changes to the WCNOC 
    organization and to the position titles and as such have no effect 
    on plant equipment or the technical qualification of plant 
    personnel.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. This change is administrative in nature and does not 
    involve any change to the installed plant systems or the overall 
    operating philosophy of Wolf Creek Generating Station.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety. This change does not involve any changes in 
    overall organizational commitments. A position title change alone 
    does not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: Theodore R. Quay
    
    Peviously Published Notices Of Consideration Of Issuance Of 
    Amendments ToFacility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IllinoisDocket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: June 3, 1994
        Description of amendment request: In a letter of August 13, 1993, 
    and as supplemented on September 15, 1993, September 16, 1993, December 
    17, 1993, January 19, 1994, February 11, 1994, and February 24, 1994, 
    Commonwealth Edison Company submitted requests for amendments for steam 
    generator (SG) tube sleeving in accordance with (1) Westinghouse and 
    (2) Babcock & Wilcox processes. By letter dated March 4, 1994, the NRC 
    granted the proposed sleeving methods contingent upon four conditions 
    which the licensee accepted in their letter of February 24, 1994.
        Three of the four changes will be reflected in the plants' 
    Technical Specifications (TS). By letter dated June 3, 1994, the 
    licensee requested changes to TS 3.4.5 and 3.4.6.2 to include the three 
    conditions, which are:
        1. Amend the Byron and Braidwood licenses to reflect a primary-to-
    secondary leakage rate limit of 150 gallons per day (gpd) through any 
    one SG.
        2. Amend the Byron and Braidwood licenses to reflect an inservice 
    inspection of a minimum of 20 percent of a random sample of the sleeves 
    for axial and circumferential indication at the end-of-cycle. In the 
    event that an imperfection of 40 percent or greater depth is detected, 
    an additional 20 percent (minimum) of the unsampled sleeves should be 
    inspected, and if an imperfection of 40 percent or greater depth is 
    detected in the second sample, all remaining sleeves should be 
    inspected.
        3. Add a condition to the Byron and Braidwood licenses to conduct 
    additional corrosion testing to establish the design life for the 
    kinetically or laser welded sleeved tubes in the presence of a crevice.
        Collectively, these conditions will enable the licensee to have:
        1. Further assurance that the integrity of the SGs will be 
    maintained in the event of a main steam line break or under loss-of-
    coolant accident (LOCA) conditions;
        2. Increased monitoring of the SG tube sleeves for any degradation; 
    and
        3. Increased confidence that SG sleeve integrity will be maintained 
    for extended operations.
        Date of publication of individual notice in Federal Register: 
    October 12, 1994 (59 FR 51613)
        Expiration date of individual notice: November 14, 1994
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois
    
        Date of amendment request: September 7, 1994, and September 17, 
    1994 (two letters)
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to incorporate a 1.0 volt 
    steam generator tube interim plugging criteria (IPC) for Unit 1 
    beginning with Cycle 7, which has begun. This supplements the 
    information that was published in the Federal Register on August 31, 
    1994 (59 FR 45019).
        Date of publication of individual notice in Federal Register: 
    September 23, 1994 (59 FR 48917)
        Expiration date of individual notice: October 24, 1994
        Local Public Document Room location: Byron Public Library, 109 N. 
    Franklin, P.O. Box 434, Byron, Illinois 61010.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: September 16, 1994
        Brief description of amendment request: The application changes the 
    Technical Specifications pertaining to the extension of the snubber 
    functional testing interval and the increase in sample plan size.
        Date of publication of individual notice in Federal Register: 
    September 30, 1994 (59 FR 50019)
        Expiration date of individual notice: October 31, 1994
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Power Authority of the State of New York, Docket Nos. 50-286 and 
    50-333, Indian Point Nuclear Generating Unit No. 3, Westchester 
    County, New York, and James A. FitzPatrick Nuclear Power Plant, 
    Oswego County, New York
    
        Date of amendments request: September 16, 1994
        Brief description of amendments: The proposed amendments would 
    revise Section 6.0 (Administrative Controls) of the Technical 
    Specifications of both facilities to reflect, in part, licensee 
    management changes. Specifically, the title of Executive Vice 
    President-Nuclear Generation is being changed to Executive Vice 
    President and Chief Nuclear Officer and a new position, Vice President 
    Regulatory Affairs and Special Projects, which will report to the 
    Executive Vice President and Chief Nuclear Officer, is being 
    established. In addition, the list of Safety Review Committee (SRC) 
    members is being deleted and replaced with a description of SRC 
    membership requirements, including individual qualifications. Each SRC 
    member, including the alternates, will have to be approved by the 
    Executive Vice President and Chief Nuclear Officer.
        Date of publication of individual notice in Federal Register : 
    September 30, 1994 (59 FR 50021)
        Expiration date of individual notice: October 31, 1994
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601 and the Penfield 
    Library, State University of New York, Oswego, New York 13126.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New 
    YorkDate of application for amendment: September 29, 1994
    
        Brief description of amendment: The proposed amendment would revise 
    Section 4.4 of the Indian Point Nuclear Generating Unit No. 3 Power 
    Plant Technical Specifications. Specifically, TS 4.4.E.1 would be 
    revised to allow a one-time extension to the 30-month interval 
    requirement for leak rate testing of Residual Heat Removal (RHR) 
    containment isolation valves AC-732, AC-741, AC-MOV-743, AC-MOV-744, 
    and AC-MOV-1870. A one-time schedular exemption from plant specific 
    requirements associated with 10 CFR Part 50, Appendix J, Type C testing 
    (local leak rate test) for the above listed RHR containment isolation 
    valves will be processed separately. This one-time extension for leak 
    rate testing of the RHR valves would defer the leak rate testing until 
    the next refueling outage, when the RHR system can be removed from 
    service as required by current procedures.
        Date of publication of individual notice in Federal Register: 
    October 5, 1994 (59 FR 50777)
        Expiration date of individual notice: November 4, 1994
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit 2, Somervell County, Texas
    
        Date of amendment request: September 19, 1994
        Brief description of amendment request: The proposed amendment 
    would revise the technical specifications for Comanche Peak Steam 
    Electric Station Unit 2 to allow a one-time extension of emergency 
    diesel generator and related surveillance testing from 18 to 24 months.
        Date of individual notice in Federal Register: September 30, 1994 
    (59 FR 50024)
        Expiration date of individual notice: October 31, 1994
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P. O. Box 
    19497, Arlington, Texas 76019
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: September 19, 1994
        Brief description of amendment request: The proposed amendment 
    would revise the 18-month surveillance requirements of the technical 
    specifications for certain emergency core cooling system, containment 
    system, and plant systems to eliminate the restriction that these 
    surveillances be performed during shutdown or during the refueling mode 
    or cold shutdown.Date of individual notice in Federal Register: 
    September 30, 1994 (59 FR 50022)
        Expiration date of individual notice: October 31, 1994
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P. O. Box 
    19497, Arlington, Texas 76019
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: February 18, 1994, as 
    supplemented June 20, 1994
        Brief description of amendments: These amendments allow credit to 
    be taken for burnup of spent fuel assemblies in establishing storage 
    locations within the spent fuel storage pool. The current spent fuel 
    storage pool is configured to store fresh fuel assemblies with a 
    maximum radially average enrichment of 4.30 weight percent (w/o) U-235 
    in a two-out-of-four checkerboard array. These amendments allow for 
    three distinct storage regions. Region 1 allows storage of fresh fuel 
    assemblies with a maximum radially averaged enrichment equal to 4.30 w/
    o U-235 in a checkerboard configuration. Region 2 allows storage of 
    spent fuel assemblies in a three-out-of-four configuration. Region 3 
    allows storage of spent fuel assemblies in every location (four-out-of-
    four configuration).
        Date of issuance:  September 30, 1994Effective date: September 30, 
    1994
        Amendment Nos.: 82, 69, and 54
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17593) The supplemental letter dated June 20, 1994, responded to a 
    staff request for additional information, was clarifying in nature, and 
    did not affect the staff's initial no significant hazards 
    determination.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 30, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: August 18, 1994
        Brief description of amendments: These amendments revised Technical 
    Specification 6.9.1.10 to add the analytical method supplement entitled 
    ``Calculative Methods for the CE Large Break LOCA Evaluation Model for 
    the Analysis of CE and W Designed NSSS,'' CENPD-132, Supplement 3-P-A, 
    dated June 1985. This TS contains the list of analytical methods used 
    to determine the Palo Verde Nuclear Generating Station core operating 
    limits. Additionally, the existing references to earlier versions of 
    CENPD-132, and the associated approval letters are deleted.
    
        Date of issuance: October 7, 1994
        Effective date: October 7, 1994
        Amendment Nos.: 83, 70, and 55
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 6, 1994 (59 
    FR 46069) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 7, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IllinoisDocket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: July 6, 1994
        Brief description of amendments: The NRC previously approved the 
    application of steam generator tube sleeving technologies through the 
    reference of specific vendor technical reports. These amendments remove 
    specific vendor technical report references and replace them with 
    references to the generic reports.
        Date of issuance: September 29, 1994
        Effective date: September 29, 1994
        Amendment Nos.: 64, 64, 55, and 54
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39582) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 29, 1994. No 
    significant hazards consideration comments received: No
        Local Public Document Room location:  For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: August 11, 1994
        Brief description of amendment: The amendment revises Technical 
    Specification Section 6.5.1, Station Nuclear Safety Committee (SNSC), 
    to change the designation of the SNSC Chairman and to clarify the 
    maximum number of alternate members allowed for quorum purposes.
        Date of issuance: October 3, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 177
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45002) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 3, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of application for amendment: June 11, 1993, as supplemented 
    July 1, 1993, and August 11, 1994.
        Brief description of amendment: The amendment add acceptance 
    criteria for the electric and diesel fire pumps based on Emergency Core 
    Cooling System performance requirements and removes a portion of the 
    fire protection requirements from the Technical Specifications.
        Date of issuance: September 30, 1994
        Effective date: September 30, 1994
        Amendment No.: 114
        Facility Operating License No. DPR-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36432). The July 1, 1993, and August 11, 1994, letters provided 
    clarifying information within the scope of the initial notice and did 
    not affect the staff's proposed no significant hazards considerations 
    findings. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 30, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: May 24, 1994, as supplemented 
    August 4 and September 8, 1994
        Brief description of amendments: The amendments transfer the boron 
    concentration in Technical Specification (TS) 3.9.1 for the reactor 
    coolant system and the refueling canal during MODE 6, and the boron 
    concentration in TS 4.7.13.3 for the spent fuel pool from the TS to the 
    Core Operating Limits Report (COLR). The associated Bases to the TS are 
    also changed. The application is submitted in response to the guidance 
    in Generic Letter 88-16 which addresses the transfer of fuel cycle-
    specific parameter limits from the TS to the COLR.
        Date of issuance: October 7, 1994
        Effective date: To be implemented within 30 days from the date of 
    issuance
        Amendment Nos.: 125 and 119
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45022) The August 4 and September 8, 1994 supplemental submittals 
    provided clarifying information which did not affect the initial no 
    significant hazards determination. The Commission's related evaluation 
    of the amendments is contained in a Safety Evaluation dated October 7, 
    1994. No significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: May 24, 1994 as supplemented 
    August 4 and September 8, 1994.
        Brief description of amendments: The amendments transfer the boron 
    concentration values in TS 3.9.1 for the reactor coolant system and the 
    refueling canal during MODE 6, and the boron concentration value in TS 
    3/4.9.12 for the spent fuel pool from the TS to the Core Operating 
    Limits Report (COLR). The application is submitted in response to the 
    guidance in Generic Letter 88-16 which addresses the transfer of fuel 
    cycle-specific parameter limits from the TS to the COLR.
        Date of issuance: October 12, 1994
        Effective date: October 12, 1994
        Amendment Nos.: 149 and 131
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 22, 1994, 59 FR 
    32228 The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 12, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: May 12, 1994, as supplemented 
    September 2, 1994
        Brief description of amendment: The amendment revises Technical 
    Specification Sections 3.1 and 4.1 for Protective Instrumentation, the 
    associated bases, and tables to increase the surveillance test 
    intervals and add allowable out-of service times. The Technical 
    Specification changes will permit specified Channel Tests to be 
    conducted quarterly rather than weekly or monthly. The amendment will 
    enhance operational safety by reducing (1) the potential for 
    inadvertent plant scrams, (2) excessive test cycles or equipment, and 
    (3) the diversion of plant personnel and resources on unnecessary 
    testing.
        Two additional technical changes have been incorporated. The fist 
    change involves extending the Channel Calibration interval for Average 
    Power Range Monitor. The second change would add a quarterly Channel 
    Calibration requirement for High Drywell Pressure (for Core Cooling) 
    and Turbine Trip Scram Instrumentation.
        Editorial changes have been incorporated in Instrumentation 
    Sections 3.1 and 4.1 to provide clarity and consistency.
        Date of issuance: October 11, 1994
        Effective date: As of the date of issuance to be implemented within 
    90 days.
        Amendment No.: 171
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 22, 1994 (59 FR 
    32228). The September 2, 1994, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.The Commission's related evaluation 
    of this amendment is contained in a Safety Evaluation dated October 11, 
    1994.No significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Florida Power and Light Company, et al., Docket No. 50-335 St. 
    Lucie Plant, Unit No. 1, St. Lucie County, Florida
    
        Date of application for amendments: February 22, 1994
        Brief description of amendments: This amendment modifies the 
    minimum stored borated water inventory requirements for Operational 
    Modes 1 through 4 by revising Figure 3.1-1 and Limiting Condition for 
    Operation 3.1.2.8 of the unit Technical Specifications (TS). The 
    associated bases for TS 3/4.1.2 are also revised to reflect the 
    bounding borated water makeup volumes, as a function of boric acid 
    concentration, which define the proposed inventory requirements.
        Date of issuance: October 7, 1994
        Effective date: October 7, 1994
        Amendment No.: 129
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14888) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 7, 1994No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: July 19, 1994
        Brief description of amendments: The amendments relocate certain 
    cycle-specific parameter limits from the Technical Specifications to 
    the Core Operating Limits Report.
        Date of issuance: October 12, 1994
        Effective date: October 12, 1994
        Amendment Nos. 167 and 161Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39587) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 12, 1994No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of application for amendment: June 18, 1993, as supplemented 
    on December 17, 1993, and May 5, 1994.
        Brief description of amendment: The amendment would revise the 
    Technical Specifications (TS) by clarifying TS wording for the Low 
    Pressure Coolant Injection (LPCI) and Containment Spray modes of the 
    Residual Heat Removal (RHR) system to assure consistency with 
    requirements of DAEC Updated Safety Analysis Report.
        Date of issuance: October 4, 1994
        Effective date: date of issuance to be implemented within 90 days 
    of issuance.
        Amendment No.: 200
        Facility Operating License No. DPR-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37074). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 4, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: February 26, 1993 (License Amendment 
    Request 93-01), as modified by letter dated March 11, 1994, and April 
    7, 1993 (License Amendment Request 93-02), as modified by letter dated 
    February 24, 1994.
        Description of amendment request: This amendment revises the 
    Appendix A Technical Specifications relating to the operability 
    requirements for the primary component cooling water (PCCW) system, the 
    service water (SW) system, and the ultimate heat sink (UHS). The 
    amendment redefines the requirements for operable PCCW and SW systems 
    and combines the technical specification requirements for the SW system 
    and the UHS. The changes affect Technical Specification sections 3/4 
    7.3, 3/4.7.4, and 3/4.7.5.
        Date of issuance: October 5, 1994
        Effective date: October 5, 1994
        Amendment No.: 32
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notices in Federal Register: April 28, 1993 (58 FR 
    25860) June 23, 1993 (58 FR 34082). North Atlantic's letters dated 
    March 11, 1994 and February 24, 1994, provide additional clarifying 
    information related to risk calculations but neither letter changes the 
    initial proposed no significant hazards consideration determinations. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated October 5, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 47 
    Front Street, Exeter, NH 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: May 6, 1994, as supplemented 
    August 16, 1994.
        Brief description of amendment: The amendment modifies the Limiting 
    Conditions for Operation (LCO) for the Millstone Unit 2 Technical 
    Specifications (TS) 3.8.2.3 and 3.8.2.4 and the Surveillance 
    Requirements of TS 4.8.2.3.2.c.3. These changes relate to the amperage 
    requirements and the charging capability of the DC distribution 
    systems.
        Date of issuance: October 14, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 180
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 22, 1994 (59 FR 
    32232) The August 16, 1994, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated October 14, 1994. 
    No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: July 1, 1994
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) associated with the sump recirculation actuation 
    signal. The changes will be implemented after the installation of four 
    auctioneered power supplies in the Engineering Safety Feature Actuation 
    System sensor cabinets.
        Date of issuance: October 7, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 179
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42342). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 7, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: April 23, 1994, as supplemented 
    August 4, 1994
        Brief description of amendments: The amendments modify the 
    requirement for individuals filling certain plant management positions 
    to hold a Senior Reactor Operator (SRO) license. The amendments require 
    that only the Superintendent - Operations or the Assistant 
    Superintendent - Operations hold an SRO license.
        Date of issuance: September 30, 1994
        Effective date: September 30, 1994Amendment Nos. 80 and 41
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34086) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 30, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location:  Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company,Delmarva Power and Light Company, and Atlantic City 
    Electric Company,Docket No. 50-277, Peach Bottom Atomic Power 
    Station,Unit No. 2, York County, Pennsylvania
    
        Date of application for amendment: May 13, 1994, as supplemented by 
    letter dated August 28, 1994
        Brief description of amendment: This amendment allows a one-time 
    schedular extension of the second Type A Containment Integrated Leakage 
    Rate Test 10-year service period and an extended interval between Type 
    A tests.
        Date of issuance: September 30, 1994
        Effective date: September 30, 1994
        Amendment No.: 196
        Facility Operating License No. DPR-44: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 22, 1994 (59 FR 
    32235) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 30, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company,Delmarva Power and Light Company, and Atlantic City 
    Electric Company,Docket Nos. 50-277 and 50-278, Peach Bottom Atomic 
    Power Station,Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: June 9, 1994, as supplemented 
    by letter dated September 23, 1994.
        Brief description of amendments: These amendments revise the 
    Technical Specifications (TS) surveillance requirements for scram 
    insertion times. The changes make the TS similar to those described in 
    NUREG-1433, ``Standard Technical Specifications General Electric 
    Plants, BWR/4.''
        Date of issuance: September 30, 1994
        Effective date: September 30, 1994
        Amendments Nos.: 197 and 200
        Facility Operating License Nos. DPR-44 and DPR-56: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37080) The September 23, 1994 letter provided clarifying information 
    that deletes language specifying the location for scram time acceptance 
    criteria and did not change the initial proposed no significant hazards 
    consideration. The Commission's related evaluation of the amendments is 
    contained in a SafetyEvaluation dated September 30, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York 
    Date of application for amendment: November 17, 1993, as 
    supplemented August 9, 1994
    
        Brief description of amendment: The amendment revised the Technical 
    Specifications (TSs) to incorporate an instrument calibration 
    ``allowable value'' format instead of the previous ``setting limit'' 
    format. Instrumentation requiring specific value changes in the TSs 
    included:
        (1) The overpressure protection system (OPS) actuation curve (TS 
    Figure 3.1.A-3).
        (2) The minimum refueling water storage tank (RWST) water volumes 
    and low level alarm settings (specified in TS Section 3.3.A). In 
    addition the RWST level indicating switch calibration frequency 
    (specified in TS Table 4.1-1) was changed from once every 18 months to 
    once every 6 months.
        (3) The control room ammonia and chlorine toxic gas instrument 
    settings (specified in TS Section 3.3.H).
        (4) The containment pressure high and high-high engineered safety 
    features instrument settings (specified in TS Table 3.5.1).(5)
        The main steam flow engineered safety features instrument settings 
    (specified in TS Table 3.5.1).
        In addition, the TS Bases for protective instrumentation limiting 
    safety system settings (specified in TS Section 2.3) were revised to 
    clarify the description on constants K through K6 which are used 
    in the overtemperature delta-temperature and overpower delta-
    temperature settings.
        Date of issuance: October 7, 1994
        Effective date: As of the date of issuance to be implemented prior 
    to restart from the current outage.
        Amendment No.: 154
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67860) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 7, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: July 25, 1994
        Brief description of amendment: The Technical Specifications 
    amendment revised Table 3.6-1 (Non-Automatic Containment Isolation 
    Valves Open Continuously or Intermittently for Plant Operation) and 
    Table 4.4-1 (Containment Isolation Valves) to delete valves SI-1833A 
    and B and add valves SI-MOV-1835A and B. The valves being deleted no 
    longer perform a containment isolation function as a result of a 
    modification which removed the boron injection tank. The valves being 
    added are needed for testing the safety injection pumps.
        Date of issuance: October 5, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 152
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42346) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 5, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: August 4, 1994
        Brief description of amendment: The amendment revises the fuel oil 
    availability requirements for the Emergency Diesel Generators (EDGs) 
    from Section 3.7 of the Technical Specifications (TSs). This TS change 
    requires that 30,026 gallons of fuel oil be available onsite in 
    addition to the oil in the EDG storage tanks. Specification 3.7.F.4 is 
    also being changed to require a total of 7056 gallons of fuel in the 
    EDG fuel oil storage tanks. In addition, administrative changes will 
    remove the word ``available'' from the phrase ''... gallons of fuel 
    available...'' in Section 3.7.A.5 (for the individual storage tanks) to 
    avoid confusion regarding the amount of usable fuel in the tanks.
        Date of issuance: October 7, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 153
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45031) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 7, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York 
    Date of application for amendment: August 4, 1994
    
        Brief description of amendment: The amendment revises Sections 3.4 
    and 3.5 of the Technical Specifications (TSs). The TS Section 3.4 
    revision reduces the maximum allowable percent of rated power 
    associated with inoperable Main Steam Safety Valves (MSSVs). This 
    change modifies Table 3.4-1 and the associated basis such that the 
    maximum power level allowed for operation with inoperable MSSVs is 
    below the heat removing capability of the operable MSSVs. The TS 
    Section 3.5 revision corrects administrative errors in the action 
    statements associated with Items 2.a and 2.c of Table 3.5-4. 
    Additionally, the changes to Item 2.b of Table 3.5-3 and Item 2.b of 
    Table 3.5-4 clarify the action statements associated with inoperable 
    high containment pressure (Hi-Hi Level) instrumentation.
    
        Date of issuance:   October 3, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 151
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45031) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 3, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, OhioDate of 
    application for amendment: September 3, 1992, as supplemented on 
    August 22, 1994
    
        Brief description of amendment: The amendment revises the Technical 
    Specifications to include the maximum allowable steam generator level 
    as a variable limit based on the plant's mode of operation for Modes 1-
    4 and to include additional shutdown margin requirements in Mode 3. The 
    amount of main steam superheat, the status of the main feedwater pumps, 
    and the status of the Steam and Feedwater Rupture Control System were 
    considered in determining the appropriate limits for the maximum 
    allowable steam generator level.
        Date of issuance: October 7, 1994
        Effective date: October 7, 1994
        Amendment No. 192
        Facility Operating License No. NPF-3. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 28, 1992 (57 FR 
    48830) The August 22, 1994, submittal, provided additional supplemental 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    October 7, 1994.No significant hazards consideration comments received: 
    No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, OhioDate of 
    application for amendment: March 30, 1994
    
        Brief description of amendment: Revise T.S. to increase the 
    required boration flowrate in the event the required shutdown margin is 
    not met; increase the applicable minimum boron concentration and/or 
    volume requirements; revise the applicable Action statements and 
    surveillance requirements, and propose several administrative and 
    editorial changes.
        Date of issuance: September 29, 1994
        Effective date: date of issuance, to be implemented within 90 days
        Amendment No. 191
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27067) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 29, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: November 15, 1993
        Brief description of amendments: The amendments revise the Comanche 
    Peak Steam Electric Station Units 1 and 2 technical specifications by 
    increasing the maximum permitted power at which the post-refueling 
    power ascension reactor coolant system flow verification can be 
    performed.
        Date of issuance: October 7, 1994
        Effective date: October 7, 1994, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 30; Unit 2 - Amendment No. 
    15
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17606) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 7, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: March 28, 1994
        Brief description of amendments: The amendments revise the 
    technical specifications by deleting reference to a large break LOCA 
    analysis methodology that is no longer applicable, and adding reference 
    to an approved steamline break analysis methodology.
        Date of issuance: October 5, 1994
        Effective date: October 5, 1994, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 28; Unit 2 - Amendment No. 
    14
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37088) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 5, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: April 25, 1994
        Brief description of amendments: The amendments revise the TS 
    Surveillance Requirement 4.8.1.1.2 to allow ``slow starts'' of the 
    emergency diesel generator (EDG) instead of ``fast starts'' during the 
    monthly surveillance. A ``fast start'' is still required to be 
    performed at least once every 184 days. These changes are expected to 
    improve EDG availability and reliability.
        Date of issuance: October 6, 1994
        Effective date: October 6, 1994, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 29; Unit 2 - Amendment No. 
    15
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39599) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 6, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: April 15, 1994
        Brief description of amendments: The amendments modify the 
    pressure/temperature operating limitations during heatup and cooldown 
    and the Low Temperature Overpressure Protection System pressure 
    setpoints and enabling temperatures for Units 1 and 2. The proposed 
    changes include revised Limiting Conditions for Operation, Action 
    Statements, and Surveillance Requirements for the power-operated relief 
    valves and block valves to address the concerns discussed in NRC 
    Generic Letter 90-06. The proposed changes also include several 
    editorial/administrative changes.
        Date of issuance: October 5, 1994
        Effective date: October 5, 1994
        Amendment Nos.: 189 and 170
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27069) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 5, 1994No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    NuclearPower Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: May 26, 1994
        Brief description of amendment: The amendment revises the Kewaunee 
    Nuclear Power Plant (KNPP) Technical Specification (TS) Sections 2.3, 
    3.6, and 4.6, by correcting minor typographical errors and format 
    inconsistencies. These changes are being made as a part of the 
    licensee's ongoing effort to revise each section of the KNPP TS to 
    achieve a consistent format and to convert the entire document to Word 
    Perfect. In addition, changes to the basis for TS Sections 2.3, 3.6, 
    and 4.6 have been made.
    
        Date of issuance:   September 29, 1994
        Effective date:  date of issuance, to be implemented within 30 days
        Amendment No.:  111
        Facility Operating License No. DPR-43. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39601) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 29, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: May 30, 1991, as supplemented 
    May 7, 1993, and April 28, 1994.
        Brief description of amendments: These amendments revised Technical 
    Specifications 15.3.1.A.5 and 15.3.15, and Table 15.4.1-1 and 15.4.1-2. 
    The changes specified more stringent limiting conditions for operation 
    and surveillance requirements for pressurizer power-operated relief 
    valves and block valves. These changes were proposed to conform to the 
    NRC's plan for resolution of Generic Issue 70, ``Power-Operated Relief 
    Valve and Block Valve Reliability,'' and Generic Issue 94, ``Additional 
    Low-Temperature Overpressure Protection for Light Water Reactors,'' as 
    conveyed in Generic Letter 90-06. Other related changes were also made.
        Date of issuance: September 30, 1994
        Effective date: September 30, 1994, to be implemented within 90 
    days.
        Amendment Nos.: 155 & 159
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 28, 1993 (58 FR 
    16233). The May 7, 1993, and April 28, 1994, letters provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination.The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated September 30, 1994. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By November 25, 1995, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Arizona Public Service Company, et al., Docket No. STN 50-529, Palo 
    Verde Nuclear Generating Station, Unit No. 2, Maricopa County, 
    Arizona
    
        Date of amendment for amendment: October 9, 1994, as supplemented 
    by letter dated October 12, 1994
        Brief description of amendment: The proposed amendment would modify 
    Technical Specification (TS) 4.8.2.1.e, ``DC Sources - Operating'' to 
    specify that the provisions of TS 4.0.1 and 4.0.4 are not applicable to 
    the battery capacity requirements until entry into Mode 4 coming out of 
    the fifth refueling outage or upon any deep discharge cycle of the 
    battery. The amendment was requested on an emergency basis so that the 
    licensee could declare the Unit 2 batteries operable based upon the 
    current capacities of the batteries without having to satisfy the 
    surveillance requirement of TS 4.8.2.1.e. The licensee will thus be 
    able to change modes and start up from the current mid-cycle steam 
    generator inspection outage.
        Date of issuance: October 13, 1994
        Effective date: October 13, 1994
        Amendment No.: 71
        Facility Operating License No. NPF-51: The amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No.The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated October 13, 1994.
        Local
        Public Document Room location: Phoenix Public Library, 12 East 
    McDowell Road, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: Theodore R. Quay
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County,North Carolina
    
        Date of application for amendments: September 9, 1994
        Brief description of amendments: The amendments change the 
    Technical Specifications (TS) to revise the frequency for verifying the 
    position of the drywell-suppression chamber vacuum breakers when a 
    valve position indicator is inoperable from at least once every 72 
    hours to at least once every 14 days.
        Date of issuance: October 5, 1994
        Effective date: October 5, 1994
        Amendment Nos.: 172 and 203
        Facility Operating License Nos. DPR-71 and DPR-62. Amendments 
    revise the Technical Specifications.Public comments requested as to 
    proposed no significant hazards consideration: Yes. (59 FR 47648 dated 
    September 16, 1994) That notice provided an opportunity to submit 
    comments on the Commission's proposed no significant hazards 
    consideration determination. No comments have been received. The notice 
    also provided for an opportunity to request for a hearing by October 3, 
    1994, but indicated that if the Commission makes a final no significant 
    hazards determination, any such hearing would take place after issuance 
    of the amendment. The Commission's related evaluation of the amendments 
    and final no significant hazards consideration determination are 
    contained in a Safety Evaluation dated October 5, 1994.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: Mr. Mark S. Calvert, Associate General 
    Counsel, Carolina Power & Light Company, Brunswick Steam Electric 
    Plant, P. O. Box 10429, Southport, North Carolina 28461
        NRC Project Director: Michael L. Boyle
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: September 12, 1994, as supplemented 
    September 30, 1994.
        Brief description of amendment: The amendment revises technical 
    specification 3/4.2.2, ``APRM Setpoints,'' to permit operation in 
    accordance with the Boiling Water Reactor Owners' Group (BWROG) 
    guidelines on improved BWR thermal-hydraulic stability.
        Date of issuance: October 7, 1994
        Effective date: October 7, 1994
        Amendment No.: 75
        Facility Operating License No. NPF-47. The amendment revised the 
    Technical Specifications. Public comments requested to proposed no 
    significant hazards consideration: Yes, September 21, 1994 (59 FR 
    48456). The Commission's related evaluation of the amendment, and final 
    determination of no significant hazards consideration are contained in 
    a Safety Evaluation dated October 7, 1994.Attorney for the licensee: 
    Mark Wetterhahn, Esq., Winston & Strawn, 1400 L Street, NW., 
    Washington, D.C. 20005
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
        NRC Project Director: William D. Beckner
        Dated at Rockville, Maryland, this 19th day of October, 1994.
        For The Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II Office of Nuclear Reactor 
    Regulation
    [Doc. 94-26422 Filed 10-25-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
10/26/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
X94-11026
Dates:
September 30, 1994
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: October 26, 1994