95-24553. The Cleveland Electric Illuminating Company, et al.; Perry Nuclear Power Plant, Unit No. 1; Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 60, Number 191 (Tuesday, October 3, 1995)]
    [Notices]
    [Pages 51820-51821]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-24553]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket No. 50-440]
    
    
    The Cleveland Electric Illuminating Company, et al.; Perry 
    Nuclear Power Plant, Unit No. 1; Environmental Assessment and Finding 
    of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of several exemptions from the requirements of 10 
    CFR Part 50, Appendix J to the Cleveland Electric Illuminating Company, 
    Centerior Service Company, Duquesne Light Company, Ohio Edison Company, 
    Pennsylvania Power Company, and Toledo Edison Company (the licensees), 
    for operation of the Perry Nuclear Power Plant, Unit 1, located in Lake 
    County, Ohio.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed action would grant exemptions from the requirements of 
    Sections III.A.5(b)(2), III.B.3, III.C.3, III.A.1(d), III.D.1(a), and 
    III.D.3 of Appendix J to 10 CFR Part 50. Section III.A.5(b)(2) requires 
    that the measured leakage for the containment integrated leak rate test 
    (Lam) be less than 75% of the maximum allowable leakage rate (0.75 
    La). The proposed exemption would permit separate treatment of 
    main steam isolation valve leakage from the containment integrated leak 
    rate tests.
        Sections III.B.3 and III.C.3 require that the combined leakage of 
    valves and penetrations subject to Type B and C local leak rate testing 
    be less than 0.6 times the maximum allowable leakage rate (0.6 
    La). The proposed exemption would permit separate treatment of 
    main steam isolation valve leakage from local leak rate testing.
        Section III.A.1(d) requires that all fluid systems that would be 
    open to containment following post-accident conditions, be vented and 
    drained prior to conducting the containment integrated leak rate test. 
    The proposed exemption would permit separate treatment of the main 
    steam line penetrations and would not require them to be vented and 
    drained prior to conducting containment integrated leak rate tests.
        Section III.D.1.(a) requires that a set of three Type A tests be 
    performed at approximately equal intervals during each 10-year service 
    period and that the third test of each set be conducted when the plant 
    is shut down for the 10-year plant inservice inspection (ISI). The 
    proposed exemption would permit performance of the third Type A test at 
    times other than when the plant is shut down for the 10-year plant ISI.
        Section III.D.3 requires that Type C tests shall be performed 
    during each reactor shutdown for refueling but in no case at intervals 
    greater than 2 years. The proposed exemption would allow the licensee 
    to perform the required Type C tests while the plant is at power.
        The proposed action is in accordance with the licensee's 
    application for exemption dated October 21, 1994.
    
    The Need for the Proposed Action
    
        Assumptions used in both the Perry FSAR and Standard Review Plan 
    15.6.5, Appendix D, ``Radiological Consequences of a Design Basis Loss-
    of-Coolant Accident,'' for computing the total radiological 
    consequences from a hypothetical loss-of-coolant accident (LOCA), 
    include separate contributions for the containment leak rate and the 
    main steam line isolation valve leak rate. The value for the maximum 
    allowable containment leak rate, La, of 0.2%/day, was established 
    based on separate accounting for the main steam line isolation valve 
    leak rate. The proposed exemption from Section III.A.5 (b)(2) is needed 
    to allow separate treatment of main steam line isolation valve leakage 
    from the containment integrated leak rate.
        Sections III.B.3 and III.C.3 of Appendix J state that the combined 
    leakage from all valves and penetrations subject to Type B and C local 
    leak rate testing shall be less than 0.6 La. However, separate 
    leakage limits have been established for the main steam isolation 
    valves at Perry. An exemption from Sections III.B.3 and III.C.3 is 
    needed to allow separate treatment of main steam isolation valve 
    leakage from local leak rate testing.
        Section III.A.1(d) requires that those systems that would be 
    exposed to the containment atmosphere following a design basis LOCA, be 
    vented and drained prior to conducting the containment integrated leak 
    rate test. However, the main steam piping between the inboard and 
    outboard isolation valves at Perry are filled with water during the 
    containment integrated leak rate tests. This practice ensures that any 
    leakage through the isolation valves will not contribute to the overall 
    containment test results. An exemption from Section III.A.1(d) is 
    needed to allow this alternative practice.
        The proposed exemption from 10 CFR Part, Appendix J, Section 
    III.D.1(a), is needed to avoid unnecessary restraints in outage 
    scheduling. The licensee proposed to perform the three Type A tests at 
    approximately equal intervals within each 10-year period, with the 
    third test of each set conducted as close as practical to the end of 
    the 10-year period. However, there would be no required connection 
    between the Appendix J 10-year interval and the ISI 10-year interval.
        Section III.D.3 of Appendix J to 10 CFR part 50 states that Type C 
    tests shall be performed during each reactor shutdown for refueling but 
    in no case at intervals greater than 2 years. The proposed exemption is 
    needed to allow the option to perform Type C testing at power.
    
    Environmental Impacts of the Proposed Action
    
        The Commission has completed its evaluation of the proposed action 
    and concludes that the exemption would not significantly increase the 
    probability or amount of expected primary containment leakage, and that 
    containment integrity would thus be maintained.
        The change will not increase the probability or consequences of 
    accidents, no changes are being made in the types of any effluents that 
    may be released offsite, and there is no significant increase in the 
    allowable individual or cumulative occupational radiation exposure. 
    Accordingly, the Commission concludes that there are no 
    
    [[Page 51821]]
    significant radiological environmental impacts associated with the 
    proposed action.
        With regard to potential nonradiological impacts, the proposed 
    action does involve features located entirely within the restricted 
    area as defined in 10 CFR Part 20. It does not affect nonradiological 
    plant effluents and has no other environmental impact. Accordingly, the 
    Commission concludes that there are no significant nonradiological 
    environmental impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there is no measurable 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated. As an alternative to the proposed action, the staff 
    considered denial of the proposed action. Denial of the application 
    would result in no change in current environmental impacts. The 
    environmental impacts of the proposed action and the alternative action 
    are similar.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the ``Final Environmental Statement related to 
    the operation of the Perry Nuclear Power Plant, Units 1 and 2,'' dated 
    August 1982.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, on September 13, 1995, the 
    staff consulted with the Ohio state official, Lawrence Grove, of the 
    Ohio Emergency Management Agency, regarding the environmental impact of 
    the proposed action. The state official had no comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated October 21, 1994, which is available for public 
    inspection at the Commission's Public Document Room, The Gelman 
    Building, 2120 L Street, NW., Washington, DC, and at the local public 
    document room located at the Perry Public Library, 3753 Main Street, 
    Perry, Ohio 44081.
    
        Dated at Rockville, Maryland, this 26th day of September 1995.
    
        For The Nuclear Regulatory Commission.
    Jon B. Hopkins, Sr.,
    Project Manager, Project Directorate III-3, Division of Reactor 
    Projects III/IV, Office of Nuclear Reactor Regulation.
    [FR Doc. 95-24553 Filed 10-2-95; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Published:
10/03/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-24553
Pages:
51820-51821 (2 pages)
Docket Numbers:
Docket No. 50-440
PDF File:
95-24553.pdf