99-29846. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 221 (Wednesday, November 17, 1999)]
    [Notices]
    [Pages 62704-62722]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-29846]
    
    
    -----------------------------------------------------------------------
    
    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from October 23, 1999, through November 5, 1999. 
    The last biweekly notice was published on November 3, 1999 (64 FR 
    59796).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By December 17, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC, and electronically from 
    the ADAMS Public Library component on the NRC Web site, http://
    www.nrc.gov (the Electronic Reading Room). If a request for a hearing 
    or petition for leave to intervene is filed by the above date, the 
    Commission or an Atomic Safety and Licensing Board Panel, will rule on 
    the request and/or petition; and the Secretary or the designated Atomic 
    Safety and Licensing Board will issue a notice of a hearing or an 
    appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the
    
    [[Page 62705]]
    
    proceeding, a petitioner shall file a supplement to the petition to 
    intervene which must include a list of the contentions which are sought 
    to be litigated in the matter. Each contention must consist of a 
    specific statement of the issue of law or fact to be raised or 
    controverted. In addition, the petitioner shall provide a brief 
    explanation of the bases of the contention and a concise statement of 
    the alleged facts or expert opinion which support the contention and on 
    which the petitioner intends to rely in proving the contention at the 
    hearing. The petitioner must also provide references to those specific 
    sources and documents of which the petitioner is aware and on which the 
    petitioner intends to rely to establish those facts or expert opinion. 
    Petitioner must provide sufficient information to show that a genuine 
    dispute exists with the applicant on a material issue of law or fact. 
    Contentions shall be limited to matters within the scope of the 
    amendment under consideration. The contention must be one which, if 
    proven, would entitle the petitioner to relief. A petitioner who fails 
    to file such a supplement which satisfies these requirements with 
    respect to at least one contention will not be permitted to participate 
    as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and electronically from the ADAMS Public 
    Library component on the NRC Web site, http://www.nrc.gov (the 
    Electronic Reading Room).
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: October 21, 1999.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) for the Harris Nuclear Plant 
    (HNP) to implement selected improvements described in NRC Generic 
    Letter (GL) 93-05, ``Line-Item Technical Specifications To Reduce 
    Surveillance Requirements For Testing During Power Operation,'' dated 
    September 27, 1993. Specifically, HNP proposes to modify the following 
    TS to be consistent with GL 93-05: (1) TS 4.1.3.1.2--Change the 
    frequency of the control rod movement test to quarterly; (2) TS 
    4.6.4.1--Change the frequency of the Hydrogen Monitor analog channel 
    operational test to quarterly; (3) TS 4.3.3.1 (Table 4.3-3)--Change the 
    Radiation Digital Channel Operational Test to quarterly; (4) TS 
    4.4.6.2.2.b.--Change the time for remaining in cold shutdown without 
    leak testing the Reactor Coolant System Pressure Isolation Valves to 7 
    days; (5) TS 4.4.3.2--Change the testing of the capacity of pressurizer 
    heaters to once per 18 months; (6) TS 4.6.4.2.a.--Change the Hydrogen 
    Recombiner functional test to once per 18 months; and (7) TS 
    4.7.1.2.1.a--Change frequency of testing Auxiliary Feedwater Pumps to 
    quarterly.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        There are no systems being modified as a result of this change. 
    Additionally, the way in which equipment is tested is not affected 
    by this change. Reducing surveillance intervals for TS components 
    (such as control rod testing) may reduce the probability of an 
    accident (rod drop accident) by reducing actions that could cause an 
    accident to occur (rod movement).
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        No system, structure, or component is being modified as a result 
    of this change. Additionally, there are no changes to the way 
    equipment is operated as a result of this change. Operating 
    parameters are not being modified as a result of this change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        These proposed changes are in accordance with NRC Generic Letter 
    93-05, dated September 27, 1993 and NUREG-1366, dated December 1992. 
    These changes pertain to testing requirements for TS equipment which 
    help ensure operability requirements are met. This change does not 
    modify the required safety function or operating parameters for 
    equipment described in HNP TS.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: William D. Johnson, Vice President and 
    Corporate Secretary, Carolina Power & Light Company, Post Office Box 
    1551, Raleigh, North Carolina 27602.
        NRC Section Chief: Kahtan Jabbour, Acting.
    
    Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: October 15, 1999.
    
    [[Page 62706]]
    
        Description of amendment request: The amendments would revise 
    Section 5.5.7, ``Reactor Coolant Pump Flywheel Inspection Program,'' of 
    the Technical Specifications. Section 5.5.7 currently specifies that 
    inspections be done according to Regulatory Position c.4.b of 
    Regulatory Guide 1.14, Revision 1, such that an in-place ultrasonic 
    volumetric examination of the areas of higher stress concentration at 
    the bore and keyway be performed at approximately 3-year intervals. The 
    licensee proposed to revise this to require a qualified in-place 
    ultrasonic examination over the volume from the inner bore of the 
    flywheel to the circle of one half the outer radius, or a surface 
    examination (magnetic particle and/or penetration testing) of exposed 
    surfaces defined by the volume of the disassembled flywheel. The 
    licensee stated that the technical basis has been set forth in 
    Westinghouse Topical Report WCAP-14535A, and cited similar amendments 
    already granted to other nuclear plants.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    First Standard
    
        Would implementation of the changes proposed in this LAR involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated?
        No. There are no accident probabilities or consequences impacted 
    by this LAR [license amendment request]. As discussed in Attachment 
    3 [the licensee's description of the proposed amendment], following 
    a reduction in the scope and frequency of the examinations currently 
    required by the applicable Technical Specifications and Regulatory 
    Guide 1.14, Revision I, an adequate inservice inspection program 
    will continue to be maintained for the reactor coolant pump 
    flywheels. Since the integrity of the flywheels will continue to be 
    ensured, these components will continue to be available to fulfill 
    their existing design function during pump coastdown flow 
    transients. Additionally, there is no more risk that the flywheels 
    will become a source of missile generation. Consequently, there is 
    no significant increase in the probability or consequences of an 
    accident previously evaluated.
    
    Second Standard
    
        Would implementation of the changes proposed in this LAR create 
    the possibility of a new or different kind of accident from any 
    previously evaluated?
        No. The proposed changes contained in this LAR only reduce the 
    existing inspection requirements for the reactor coolant pump 
    flywheels. This LAR proposes no changes to the plants' design, 
    equipment, or method of operation at either McGuire or Catawba 
    Nuclear Station. Furthermore, the reduction in the inspection 
    requirements for the flywheels has been generically approved by the 
    NRC and is justified by WCAP-14535A. Therefore, since implementation 
    of this LAR results in no actual impact upon either of the Duke 
    nuclear plants, and since the integrity of the flywheels will 
    continue to be ensured at an acceptable level, no new or different 
    kinds of accidents are being created.
    
    Third Standard
    
        Would implementation of the changes proposed in this LAR involve 
    a significant reduction in a margin of safety?
        No. Margin of safety is related to the confidence in the ability 
    of the fission product barriers to perform their design functions 
    during and following an accident situation. These barriers include 
    the fuel cladding, the reactor coolant system, and the containment 
    system. These barriers are unaffected by the changes proposed in 
    this LAR. As discussed in WCAP-14535A, a reduction in the frequency 
    for performing the inservice inspections currently done in 
    accordance with Regulatory Guide 1.14, Revision I, will not preclude 
    the ability to accurately demonstrate the integrity of the reactor 
    coolant pump flywheels. This LAR creates no additional threat to the 
    integrity of the fission product barriers from the standpoint of 
    missile generation or otherwise. Therefore, implementation of the 
    changes proposed in this LAR does not impact the assumption of the 
    integrity of the flywheels, the fission product barriers, or any 
    other accident analyses assumptions. Consequently, no margin of 
    safety will be significantly impacted by this LAR.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Ms. Lisa F. Vaughn, Legal Department 
    (PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte, 
    North Carolina.
        NRC Section Chief: Richard L. Emch, Jr.
    
    Duke Energy Corporation, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: October 15, 1999.
        Description of amendment request: The amendments would revise 
    Section 5.5.7, ``Reactor Coolant Pump Flywheel Inspection Program,'' of 
    the Technical Specifications. Section 5.5.7 currently specifies that 
    inspections be done according to Regulatory Position c.4.b of 
    Regulatory Guide 1.14, Revision 1, such that an in-place ultrasonic 
    volumetric examination of the areas of higher stress concentration at 
    the bore and keyway be performed at approximately 3-year intervals. The 
    licensee proposed to revise this to require a qualified in-place 
    ultrasonic examination over the volume from the inner bore of the 
    flywheel to the circle of one half the outer radius, or a surface 
    examination (magnetic particle and/or penetration testing) of exposed 
    surfaces defined by the volume of the disassembled flywheel. The 
    licensee stated that the technical basis has been set forth in 
    Westinghouse Topical Report WCAP-14535A, and cited similar amendments 
    already granted to other nuclear plants.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    First Standard
    
        Would implementation of the changes proposed in this LAR involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated?
        No. There are no accident probabilities or consequences impacted 
    by this LAR [license amendment request]. As discussed in Attachment 
    3 [the licensee's description of the proposed amendment], following 
    a reduction in the scope and frequency of the examinations currently 
    required by the applicable Technical Specifications and Regulatory 
    Guide 1.14, Revision I, an adequate inservice inspection program 
    will continue to be maintained for the reactor coolant pump 
    flywheels. Since the integrity of the flywheels will continue to be 
    ensured, these components will continue to be available to fulfill 
    their existing design function during pump coastdown flow 
    transients. Additionally, there is no more risk that the flywheels 
    will become a source of missile generation. Consequently, there is 
    no significant increase in the probability or consequences of an 
    accident previously evaluated.
    
    Second Standard
    
        Would implementation of the changes proposed in this LAR create 
    the possibility of a new or different kind of accident from any 
    previously evaluated?
        No. The proposed changes contained in this LAR only reduce the 
    existing inspection requirements for the reactor coolant pump 
    flywheels. This LAR proposes no changes to the plants' design, 
    equipment, or method of operation at either McGuire or Catawba 
    Nuclear Station. Furthermore, the reduction in the inspection 
    requirements for the flywheels has been generically approved by the 
    NRC and is justified by WCAP-14535A. Therefore, since implementation 
    of this LAR results in no actual impact upon either of the Duke 
    nuclear plants, and since the integrity of the flywheels will 
    continue to be ensured at an acceptable level, no new or different 
    kinds of accidents are being created.
    
    [[Page 62707]]
    
    Third Standard
    
        Would implementation of the changes proposed in this LAR involve 
    a significant reduction in a margin of safety?
        No. Margin of safety is related to the confidence in the ability 
    of the fission product barriers to perform their design functions 
    during and following an accident situation. These barriers include 
    the fuel cladding, the reactor coolant system, and the containment 
    system. These barriers are unaffected by the changes proposed in 
    this LAR. As discussed in WCAP-14535A, a reduction in the frequency 
    for performing the inservice inspections currently done in 
    accordance with Regulatory Guide 1.14, Revision I, will not preclude 
    the ability to accurately demonstrate the integrity of the reactor 
    coolant pump flywheels. This LAR creates no additional threat to the 
    integrity of the fission product barriers from the standpoint of 
    missile generation or otherwise. Therefore, implementation of the 
    changes proposed in this LAR does not impact the assumption of the 
    integrity of the flywheels, the fission product barriers, or any 
    other accident analyses assumptions. Consequently, no margin of 
    safety will be significantly impacted by this LAR.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Mr. Albert Carr, Duke Energy Corporation, 
    422 South Church Street, Charlotte, North Carolina.
        NRC Section Chief: Richard L. Emch, Jr.
    
    Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of amendment request: September 29, 1999.
        Description of amendment request: The proposed amendments would 
    revise the Containment Inservice Inspection (ISI) Program Technical 
    Specifications (TS) 5.5.2, ``Containment Leakage Testing Program,'' and 
    TS 5.5.7, ``Pre-Stressed Concrete Containment Tendon Surveillance 
    Program.'' The proposed amendments would permit the American Society of 
    Mechanical Engineers (ASME) Boiler and Pressure Vessel Code, Section 
    XI, Subsection IWL visual examinations to be performed in lieu of 
    concrete and post-tensioning system general visual examinations 
    required by 10 CFR 50, Appendix J and Regulatory Guide 1.163 between 
    Type A tests. In addition, the amendment would permit general visual 
    examinations of the concrete and post-tensioning system that can be 
    performed with a unit in operation to be performed prior to the 
    beginning of a refueling outage during which a Type A test is 
    scheduled.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        A. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        No. Implementation of this amendment would not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated. Approval of this amendment will have 
    no significant effect on accident probabilities or consequences. The 
    containment is not an accident initiating system or structure; 
    therefore, there will be no impact on any accident probabilities by 
    the approval of this amendment. The containment serves an important 
    function to mitigate consequences of postulated accidents previously 
    evaluated and the examination frequencies proposed in this amendment 
    will not result in a reduction in the capacity of the containment to 
    meet its intended function. The requested flexibility in scheduling 
    containment visual examinations has no significant impact on the 
    validity of the examinations or of containment structural integrity.
        Additionally, the change to Technical Specification 5.5.7 and 
    the planned revision to Selected Licensee Commitment 16.6.2 
    described in this amendment application reflect the adoption of an 
    ASME Section XI, Subsection IWE and IWL Inservice Inspection Program 
    as required by 10 CFR 50 Section 55a(g)(4). Implementation of this 
    program will not result in a reduction in the capacity of the 
    containment to meet its intended function.
        Therefore, the probability or consequences of an accident 
    previously evaluated will not be increased by approval of the 
    requested changes.
        B. Create the possibility of a new or different kind of accident 
    from the accident previously evaluated?
        No. Implementation of this amendment would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. No new accident causal mechanisms are created 
    as a result of NRC approval of this amendment request. No changes 
    are being made to the plant that would introduce any new accident 
    causal mechanisms. This amendment request does not impact any plant 
    systems that are accident initiators, since the containment 
    functions primarily as an accident mitigator.
        C. Involve a significant reduction in a margin of safety?
        No. Implementation of this amendment would not involve a 
    significant reduction in a margin of safety. Margin of safety is 
    related to the confidence in the ability of the fission product 
    barriers to perform their design functions during and following an 
    accident situation, including the performance of the containment. 
    This component is already capable of performing as intended, and its 
    function is verified by visual examination, post-tensioning system 
    examinations, and leakage rate testing.
        The examination requirements of ASME XI, Subsection IWL, are 
    essentially identical to those contained in Regulatory Guide 1.35, 
    Rev. 3, and are more rigorous than those required by 10 CFR 50, 
    Appendix J and Regulatory Guide 1.163. Previous visual examinations 
    of containment concrete and post-tensioning system surfaces have not 
    revealed any indications of abnormal degradation of the containment. 
    The five-year frequency for IWL examinations is adequate in lieu of 
    the general visual examination frequency specified in Regulatory 
    Guide 1.163 for containment concrete and post-tensioning system 
    examinations.
        The ability of the containment to perform its design function 
    will not be impaired by the implementation of this amendment at 
    Oconee Nuclear Station. Consequently, no safety margins will be 
    impacted.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Anne W. Cottingham, Winston and Strawn, 1200 
    17th Street, NW., Washington, DC.
        NRC Section Chief: Richard L. Emch, Jr.
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley Power 
    Station, Unit 2, Shippingport, Pennsylvania
    
        Date of amendment request: June 17, 1999.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Section 3.4.9.1 and associated 
    figures to extend the applicability of the heatup and cooldown curve 
    pressure and temperature limits from 10 effective full power years 
    (EFPY) to 15 EFPY. The proposed changes include new heatup and cooldown 
    curves developed in accordance with the methodology provided in 
    Regulatory Guide 1.99, Revision 2, and Code Case N-640. The 
    applicability of TS Section 3.4.9.3, Overpressure Protection Systems, 
    is also updated to 15 EFPY, and the maximum allowable power operated 
    relief valve (PORV) setpoints for the over pressure protection system 
    are revised. Revisions to the TS Bases are also made.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    
    [[Page 62708]]
    
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed heatup and cooldown curves have been revised by 
    changing the applicability from 10 effective full power years (EFPY) 
    to 15 EFPY. The curves have been developed in accordance with the 
    methodology provided in Regulatory Guide 1.99, Revision 2 and Code 
    Case N-640. The proposed heatup and cooldown curves define limits 
    that still ensure the prevention of nonductile failure for the 
    reactor vessel. The design basis events that were protected against 
    have not changed; therefore, the probability of an accident is not 
    increased.
        The overpressure protection system (OPPS) has been revised such 
    that the applicability has changed from 10 EFPY to 15 EFPY. This 
    system protects the Reactor Coolant System (RCS) at low temperatures 
    so that the integrity of the Reactor Coolant Pressure Boundary 
    (RCPB) is not compromised by violating the pressure/temperature (P/
    T) limits. These changes were determined in accordance with the 
    methodologies set forth in the regulations to provide an adequate 
    margin of safety to ensure the reactor vessel will withstand the 
    effects of normal cyclic loads due to temperature and pressure 
    changes as well as the loads associated with postulated faulted 
    events. The lower limit on pressure during the design basis OPPS 
    mass injection and heat addition transients is established based on 
    operational consideration for the RCP number one seal limit which 
    requires a nominal differential pressure across the seal faces for 
    proper film-riding performance. As part of the OPPS setpoint 
    evaluation, margin to the RCP number one seal limit is evaluated.
        This limit corresponds to a differential pressure across the 
    seal of 200 psid, which corresponds to the gage pressures. The 
    pressure undershoot below the PORV setpoint during a design basis 
    mass injection or heat addition event can exceed 100 psi. Therefore, 
    with the PORV setpoints developed for the 15 EFPY heatup and 
    cooldown curves, there is the potential for RCS pressure to violate 
    the RCP number one seal limit at the lowest RCS temperatures.
        Undershoot below the PORV setpoint can be significantly higher 
    if both PORVs actuate during an OPPS event, and it is anticipated 
    that the pump seal limit would be exceeded. However, staggering the 
    setpoints minimizes the likelihood that both PORVs will actuate 
    simultaneously during credible OPPS events. Similarly, WCAP 14040-
    NP-A indicates that when there is insufficient range between the 
    upper and lower pressure limits to select PORV setpoints that 
    provide protection against violating both limits, then the setpoint 
    selection that provides protection against the upper limit violation 
    takes precedence. WCAP-4040-NP, Revision 1 was approved by the NRC 
    by letter dated October 16, 1995, which was incorporated in Revision 
    2 of the approved WCAP issued in January 1996.
        Modification of the heatup and cooldown curves and OPPS 
    setpoints does not alter any assumptions previously made in the 
    radiological consequence evaluations nor affect mitigation of the 
    radiological consequences of an accident described in the Updated 
    Final Safety Analysis Report (UFSAR). Therefore, the proposed 
    changes will not significantly increase the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed heatup and cooldown curves applicable for the first 
    15 EFPY were generated using approved methodology and Code Case N-
    640. Generating these curves with Code Case N-640 reduced the excess 
    conservatism that exists in the current curves and results in an 
    increase in the safety of the plant, as the likelihood of RCP seal 
    failures and/or fuel problems will decrease. The change does not 
    cause the initiation of any accident nor create any new single 
    failure.
        The modification of the OPPS setpoints ensures that the RCPB 
    integrity is protected at low temperatures. The new setpoints were 
    selected using conservative assumptions to ensure that sufficient 
    margin is available to prevent violation of the P/T limits due to 
    anticipated mass and heat input transients. The modification of the 
    setpoints does not change, degrade, or prevent the safe response of 
    the RCS to accident scenarios, as described in UFSAR Chapter 15. The 
    proposed change does not cause the initiation of any accident nor 
    create any new credible single failure.
        Therefore, the proposed license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The new P/T curves define the limits for ensuring prevention of 
    nonductile failure for the reactor vessel, and does not 
    significantly reduce the margin of safety for the plant. The 
    methodology provided in Code Case N-640 removed some of the excess 
    conservatism from the current Appendix G analysis. However, this 
    improved overall plant safety by expanding the operating window 
    relative to the RCP seal requirements. The probability of damaging 
    the RCP seals is reduced. Therefore, the margin of safety is not 
    significantly reduced.
        The OPPS setpoints will continue to ensure the RCS pressure 
    boundary will be protected from pressure transients. They were 
    generated using the proposed heatup and cooldown curves as input. 
    The OPPS setpoints include additional margin by including instrument 
    uncertainties not included in the current setpoints. Therefore, the 
    margin of safety is not significantly reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Section Chief: Sheri R. Peterson.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of amendment request: July 15, 1999.
        Description of amendment request: The license amendment request 
    (LAR) proposes to revise the Technical Specifications frequency for the 
    Quench and Recirculation Spray Systems nozzle air flow test from 5 
    years to 10 years. This LAR also includes a revision to correct the 
    terminology used in an action requirement as well as miscellaneous 
    editorial and format changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed extension of the testing frequency of the Quench 
    Spray and Recirculation Spray Systems' nozzles to ten years does not 
    change the way these systems are operated or their operability 
    requirements. The proposed change to the surveillance frequency of 
    safety equipment has no impact on the probability of an accident 
    occurrence nor can it create a new or different type of accident. 
    NUREG-1366, ``Improvements to Technical Specifications Surveillance 
    Requirements,'' dated December 1992, and Generic Letter 93-05, 
    ``Line Item Technical Specifications Improvements to Reduce 
    Surveillance Requirements for Testing During Power Operation,'' 
    dated September 27, 1993, concluded that the corrosion of stainless 
    steel piping is negligible during the extended surveillance interval 
    for nozzle testing. The results of the above NRC study were 
    evaluated by Duquesne Light Company and found to be applicable to 
    Beaver Valley Power Station (BVPS) Unit 1 and 2. Since the Quench 
    Spray and Recirculation Spray Systems are maintained dry, there is 
    no additional mechanism that could cause blockage of the spray 
    nozzles. Thus, the nozzles in these spray systems are expected to 
    remain operable during the ten year surveillance interval to 
    mitigate the consequence of an accident previously evaluated. No 
    obstructed or clogged spray systems' nozzles have been observed 
    during the five year frequency surveillance tests at either BVPS 
    Unit 1 or Unit 2 to date. Testing of the spray systems' nozzles at 
    the proposed reduced frequency will not increase the probability of 
    occurrence of a postulated accident or the consequences of an 
    accident previously evaluated.
        This license amendment also revises the Action criteria in the 
    BVPS Unit 1 and 2 Axial Flux Difference [AFD] technical
    
    [[Page 62709]]
    
    specification to correct the terminology referring to the Core 
    Operating Limits Report (COLR) limits. The proposed change 
    incorporates the terminology (acceptable operation limits) used in 
    the corresponding Action condition of the ISTS [Improved Standard 
    Technical Specifications]. The proposed change does not alter the 
    AFD limits specified in the COLR and the AFD specification continues 
    to assure plant operation within those limits. With AFD within the 
    acceptable operation limits specified in the COLR, the resulting 
    axial power distribution remains within the initial conditions 
    assumed in the safety analyses. Therefore, these changes will not 
    increase the probability of occurrence of a postulated accident or 
    the consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed reduced frequency testing of the Quench Spray and 
    Recirculation Spray Systems' nozzles does not change the way the 
    spray systems are operated. The reduced frequency of testing the 
    spray nozzles does not change the plant operation or system 
    readiness. The reduced frequency testing of the Quench Spray and 
    Recirculation Spray Systems' nozzles does not generate any new 
    accident precursors. Therefore, the possibility of a new or 
    different kind of accident previously evaluated is not created by 
    the proposed changes in surveillance frequency of the spray systems' 
    nozzles.
        This license amendment also revises the Action criteria in the 
    BVPS Unit 1 and 2 Axial Flux Difference technical specification to 
    correct the terminology referring to the Core Operating Limits 
    Report (COLR) limits. This addresses an incorrect use of terminology 
    and the revision does not involve a technical intent change. 
    Therefore, the possibility of a new or different kind of accident 
    previously evaluated is not created by the proposed terminology 
    correction.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed amendment does not involve revisions to any safety 
    limits or safety system setting that would adversely impact plant 
    safety. The proposed amendment does not affect the ability of 
    systems, structures or components important to the mitigation and 
    control of design bases accident conditions within the facility. In 
    addition, the proposed amendment does not affect the ability of 
    safety systems to ensure that the facility can be maintained in a 
    shutdown or refueling condition for extended periods of time.
        Reduced testing of the Quench Spray and Recirculation Spray 
    Systems' nozzles does not change the way these spray systems are 
    operated or these spray systems' operability requirements. Generic 
    Letter 93-05 and NUREG-1366 concluded that the corrosion of 
    stainless steel piping is negligible during the extended 
    surveillance interval for nozzle testing. The results of the above 
    NRC study were evaluated by Duquesne Light Company and found to be 
    applicable to BVPS Unit 1 and 2. Since the Quench Spray and 
    Recirculation Spray Systems are maintained dry, there is no 
    additional mechanism that could cause blockage of these spray 
    systems' nozzles. Thus, the proposed reduced testing frequency is 
    adequate to ensure spray nozzle operability. The surveillance 
    requirements do not affect the margin of safety in that the 
    operability requirements of the Quench Spray and Recirculation Spray 
    Systems remain unaltered. The existing safety analyses remain 
    bounding. Therefore, the margin of safety is not adversely affected.
        This license amendment also revises the Action criteria in the 
    BVPS Unit 1 and 2 Axial Flux Difference technical specification to 
    correct the terminology referring to the Core Operating Limits 
    Report (COLR) limits. This addresses an incorrect use of terminology 
    and the revision does not involve a technical intent change. The 
    operating criteria on Axial Flux Difference are not altered from 
    their intended requirements. Therefore, the margin of safety is not 
    adversely affected by the proposed terminology correction.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Sheri R. Peterson
        Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
        Date of amendment request: July 20, 1999
        Description of amendment request: The licensee amendment request 
    proposes to relocate the following Technical Specifications items to 
    the Licensing Requirements Manual:
    In-core Detectors (Unit 1 and 2),
    Chlorine Detection System (Unit 1 and 2),
    Turbine Over-speed Protection (Unit 2 only),
    Crane Travel Spent Fuel Storage Pool Building (Unit 1 and 2).
    
        In addition to the relocation, certain editorial and format changes 
    are proposed. Also, it is proposed that certain information on the 
    Remote Shutdown Panel Monitoring Instrumentation be moved to the 
    Updated Final Safety Analysis Report (USFAR).
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Consistent with the guidance provided in Generic Letter (GL) 95-
    10 and the content of the Improved Standard Technical Specifications 
    (ISTS) contained in NUREG-1431, Rev. 1, this license amendment 
    request (LAR) proposes the relocation of the following TS to the 
    Licensing Requirements Manual (LRM):
    
    3/4.3.3.2 Incore Detectors (Unit 1 and 2)
    3/4.3.3.7 Chlorine Detection System (Unit 1 and 2)
    3/4.3.4 Turbine Overspeed Protection (Unit 2 only)
    
        In order to completely relocate the chlorine detection system 
    requirements from the Technical Specifications (TS), portions of the 
    Unit 1 Specifications 3/4.7.7, Control Room Habitability Systems and 
    3/4.9.15, Control Room Emergency Habitability Systems, as well as 
    the Unit 2 Specification, 3/4.7.7, Control Room Emergency Air 
    Cleanup and Pressurization System are proposed to be revised to 
    reflect the removal of the chlorine detection system from the TS. 
    The applicable surveillance requirements, and modes of applicability 
    from these specifications are proposed to be relocated to the LRM 
    along with the associated chlorine detection system TS. In addition, 
    new actions have been added to the chlorine detection system 
    specifications to integrate the new requirements.
        In addition to the TS identified for relocation by the NRC in GL 
    95-10, this LAR proposes the relocation of another TS that does not 
    meet the criteria of 10 CFR 50.36 and is not included in the ISTS. 
    The additional TS proposed to be relocated to the LRM is 3/4.9.7 
    Crane Travel Spent Fuel Storage Pool Building (Unit 1 and 2).
        This LAR also proposes that the TS Bases section associated with 
    each of the TS listed above be relocated to the LRM as well. The 
    appropriate TS pages (i.e., LCO, Bases, Table of Contents, etc.) are 
    revised to reflect the removal of these Specifications and Bases 
    from the TS.
        The TS and bases discussed above and proposed for relocation 
    will be moved into the BVPS LRM. The Unit 1 and Unit 2 LRM are 
    appendices of the associated unit UFSAR. As part of the UFSAR any 
    changes made to the LRM must be in accordance with the provisions of 
    10 CFR 50.59.
        In addition to the relocation of the above listed TS, this LAR 
    includes the removal of the ``Measurement Range'' information from 
    the Unit 1 and 2 TS Table 3.3-9, Remote Shutdown Panel Monitoring 
    Instrumentation. This design information is being moved from the TS 
    to an applicable Updated Final Safety Analysis Report (UFSAR) 
    section. The removal of this detail from the TS is consistent with 
    the level of detail in the corresponding ISTS Specification. As part 
    of the UFSAR any changes made to the measurement range information 
    must be in accordance with the provisions of 10 CFR 50.59.
        LAR 1A-251/2A-121 includes two Bases enhancements. Additional 
    information is being added to the reactor trip system 
    instrumentation Bases to discuss diverse and anticipatory protection 
    features not credited in the accident analyses. The reactor trip 
    system instrumentation Bases is also revised
    
    [[Page 62710]]
    
    to more clearly describe the source and intermediate range neutron 
    flux protection features required during shutdown modes.
        The proposed changes include the addition of license numbers to 
    some of the TS pages contained in this LAR. In addition, this LAR 
    contains changes that update the format of the affected TS pages and 
    make editorial corrections. These changes are administrative in 
    nature and do not impact the technical content of the affected TS 
    pages.
        The proposed changes regarding the relocation of information 
    from the TS in this LAR follow the guidance provided in Generic 
    Letter 95-10, the NRC ``Final Policy Statement on Technical 
    Specifications Improvements for Nuclear Power Reactors'' (58 FR 
    39132) dated July 22, 1993, and are consistent with the content of 
    the ISTS. In addition, the proposed location for this information 
    (UFSAR and LRM) ensures that future changes to the relocated 
    requirements will be in accordance with the provisions of 10 CFR 
    50.59 and that NRC review and approval will be requested should a 
    change to this information involve an unreviewed safety question.
        The proposed amendment does not involve a significant increase 
    in the probability of an accident previously evaluated because no 
    changes are being made to any accident initiator. No analyzed 
    accident scenario is being changed. The initiating conditions and 
    assumptions for accidents described in the UFSAR remain as 
    previously analyzed. The failure of any of the systems or components 
    affected by this LAR, except for turbine overspeed protection, is 
    not an accident initiating event. Due to the low likelihood of 
    equipment damage or failure resulting from turbine missiles 
    generated by a turbine overspeed event, assumptions related to the 
    turbine overspeed protection system are not part of an initial 
    condition of a design basis accident or transient.
        The proposed amendment also does not involve a significant 
    increase in the consequences of an accident previously evaluated. 
    The amendment does not reduce the current requirements for the 
    systems and components proposed for relocation. The amendment only 
    requests that the requirements be retained in a more appropriate 
    document. The systems and components proposed for relocation in this 
    amendment perform no active role in mitigating a design basis 
    accident described in the UFSAR. The systems or components proposed 
    for relocation are not part of the initial conditions assumed in a 
    safety analysis for a design basis accident described in the UFSAR. 
    In addition, the affected systems and components do not function to 
    actuate any protective equipment, nor are they part of the primary 
    success path assumed in the safety analyses to mitigate any design 
    basis accident described in the UFSAR.
        The bases enhancements included in this LAR are administrative 
    in nature and serve only to provide additional descriptive 
    information. These changes do not impact plant safety.
        Therefore, the proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed amendment does not involve any physical changes to 
    the plant or the modes of plant operation defined in Appendix A of 
    the operating license. The proposed amendment does not involve the 
    addition or modification of plant equipment nor does it alter the 
    design or operation of any plant systems.
        Moving specifications to the LRM or design information to the 
    UFSAR will not change the physical plant or the modes of plant 
    operation. Whether these specifications are located in the TS or the 
    LRM has no effect on any previously evaluated accident. The 
    relocation of TS information does not involve a change in the 
    configuration of equipment nor does it alter the design or operation 
    of plant systems.
        Expanding the Bases for both units to discuss additional 
    information regarding the protective functions not credited in the 
    safety analysis or the neutron flux trip functions required in 
    shutdown modes provides additional information to enhance the 
    awareness of the protective instrumentation functions. The proposed 
    bases changes do not result in any adjustments or physical 
    alteration to the affected protective instrumentation functions. The 
    Reactor Protection System will continue to function as currently 
    designed and assumed in the accident analyses.
        Therefore, operation of the facility in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The margin of safety depends on the maintenance of specific 
    operating parameters and systems within design requirements and 
    safety analysis assumptions.
        The proposed amendment does not involve revisions to any safety 
    limits or safety system setting that would adversely impact plant 
    safety. The proposed amendment does not affect the ability of 
    systems, structures or components important to the mitigation and 
    control of design bases accident conditions within the facility. In 
    addition, the proposed amendment does not affect the ability of 
    safety systems to ensure that the facility can be maintained in a 
    shutdown or refueling condition for extended periods of time, and 
    sufficient instrumentation and control capability is available for 
    monitoring and maintaining the unit status.
        The relocation of TS requirements and information to the LRM or 
    UFSAR does not reduce the requirements for the affected systems and 
    components to be maintained operable and function within design 
    requirements. The relocation of TS requirements and information to 
    the LRM and UFSAR will allow changes to this information to be made 
    in accordance with the provisions of 10 CFR 50.59 and continues to 
    ensure that NRC review and approval will be requested should a 
    change to this information involve an unreviewed safety question.
        Expanding the Bases for both units to discuss additional 
    information regarding the protective functions not credited in the 
    safety analysis or the neutron flux trip functions required in 
    shutdown modes provides additional information to enhance the 
    awareness of the protective instrumentation functions. The addition 
    of descriptive text to the TS bases does not affect the TS 
    requirements for the affected equipment to be maintained operable 
    and function within the applicable design requirements. The Reactor 
    Protection System will continue to function as currently designed 
    and assumed in the accident analyses.
        Therefore, operation of the facility in accordance with the 
    proposed amendment will not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Sheri R. Peterson.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of amendment request: September 20, 1999.
        Description of amendment request: The proposed amendments would 
    revise the standard to which the control room ventilation charcoal and 
    Supplementary Leak Collection and Release System (SLCRS) charcoal must 
    be laboratory tested as specified in: Beaver Valley Power Station, Unit 
    No. 1 (BVPS-1), Technical Specification (TS) 4.7.7.1.1.c.2 for the 
    Control Room Emergency Habitability Systems; BVPS-1 TS 4.7.8.1.b.3 for 
    the SLCRS; Beaver Valley Power Station, Unit No. 2 (BVPS-2), TS 
    4.7.7.1.d for the Control Room Emergency Air Cleanup and Pressurization 
    System; and BVPS-2 TS 4.7.8.1.b.3 for the SLCRS. NRC Generic Letter 99-
    02, ``Laboratory Testing of Nuclear-Grade Activated Charcoal,'' dated 
    June 3, 1999, requested licensees to revise their TS criteria 
    associated with laboratory testing of ventilation charcoal to a valid 
    test protocol, which included American Society for Testing Materials 
    (ASTM) D3803-1989. This license amendment request revises the charcoal 
    laboratory standard to follow ASTM D3803-1989 for each BVPS Unit.
        This license amendment request also: (1) Revises the minimum amount 
    of output in kilowatts needed for the control room emergency 
    ventilation system heaters at each BVPS Unit; (2)
    
    [[Page 62711]]
    
    revises BVPS-1 SLCRS surveillance testing criteria to be consistent 
    with American National Standards Institute/American Society of 
    Mechanical Engineers (ANSI/ASME) N510-1980, the BVPS-1 control room 
    ventilation testing, and the BVPS-2 SLCRS/control room ventilation 
    testing; and (3) makes minor typographical corrections and editorial 
    changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes to the surveillance requirements for the 
    laboratory testing of ventilation system charcoal are consistent 
    with Generic Letter 99-02. The proposed change will adopt ASTM 
    D3803-1989 as the laboratory testing standard for performing the 
    surveillance associated with the Control Room emergency ventilation 
    and the SLCRS charcoal filters at each BVPS Unit. Thus this proposed 
    change will not involve a significant increase in the probability or 
    consequences of a previously evaluated accident since this standard 
    provides the assurance for continuing to comply with the current 
    BVPS Unit 1 and Unit 2 licensing basis as it relates to the dose 
    limits of GDC 19 and 10 CFR Part 100.
        The change in the control room emergency ventilation system 
    heater minimum output at both BVPS Units does not change the system 
    ability to meet its design bases. The change in the BVPS Unit 1 
    SLCRS testing frequency for adsorber/filter in-place testing and the 
    adsorber laboratory testing does not change the SLCRS system's 
    ability to meet its design bases. The change in the BVPS Unit 1 
    SLCRS testing frequency for SLCRS air flow distribution testing does 
    not change the SLCRS system's ability to meet its design bases. 
    Therefore, these changes will not increase the probability of 
    occurrence of a postulated accident or the consequences of an 
    accident previously evaluated since these systems' ability to 
    operate as required remains unchanged.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed license amendment to the control room emergency 
    ventilation system and SLCRS at both BVPS Units does not change the 
    way the system is operated. The proposed changes only involve 
    changes to the surveillance testing. These testing modifications do 
    not alter these systems' ability to perform their design bases. 
    Therefore, these proposed changes do not create the possibility of a 
    new or different kind of accident from any previously evaluated 
    accident since the control room emergency ventilation system and 
    SLCRS will continue to operate in accordance with their previous 
    design bases.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed amendment does not involve revisions to any safety 
    limits or safety system setting that would adversely impact plant 
    safety. The proposed amendment does not affect the ability of 
    system, structures or components important to the mitigation and 
    control of design bases accident conditions within the facility. In 
    addition, the proposed amendment does not affect the ability of 
    safety systems to ensure that the facility can be maintained in a 
    shutdown or refueling condition for extended periods of time.
        The proposed license amendment to the control room emergency 
    ventilation system and SLCRS at both BVPS Units does not change the 
    way the system is operated. The proposed changes only involve 
    changes to the surveillance testing. These testing modifications do 
    not alter these systems' ability to perform their design bases. The 
    existing safety analyses remain bounding. Therefore, the margin of 
    safety is not adversely affected.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Sheri R. Peterson.
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley Power 
    Station, Unit 2, Shippingport, Pennsylvania
    
        Date of amendment request: September 22, 1999.
        Description of amendment request: The proposed amendment would 
    allow a one-time only extension to the surveillance interval of 
    Technical Specification Surveillance 4.7.12.d for functional testing of 
    snubbers. The proposed extension would be limited to the end of the 8th 
    refueling outage or November 30, 2000, whichever occurs sooner.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change is for a one-time extension to the 
    surveillance interval for functional testing of snubbers specified 
    in Technical Specification (TS) 4.7.12.d. The proposed change 
    involves revising the calendar time allowed between functional tests 
    and would result in a maximum surveillance interval extension of 
    approximately 6.5 months.
        The proposed change continues to adequately limit plant 
    operation between required snubber surveillances by ensuring the 
    required surveillances are performed by November 30, 2000. 
    Therefore, the proposed change continues to limit snubber wear due 
    to vibration and elevated temperatures. The elevated temperatures 
    and vibration experienced during plant operation are the primary 
    contributors to snubber wear.
        In addition, snubber-testing experience has shown that the 
    historical failure rate of snubbers is low. There have been seven 
    refueling outages since Unit 2's startup in 1987. Only during the 
    first refueling outage, 2R01, did the snubber functional test sample 
    plan identify any inoperable snubbers. In that outage, seven 
    snubbers tested inoperable. All failed due to damage sustained 
    during original construction and startup activities. Since 2R01, no 
    inoperable snubbers were found by sample plan functional testing 
    performed during each surveillance interval. Also, the latest visual 
    inspections performed on the Unit 2 snubbers (during 2R07) revealed 
    no evidence of damage or potential problems with any snubber.
        Due to the low incidence of snubber functional test failures 
    resulting from sample plan testing and the limited plant operating 
    time between tests, the possibility of a snubber failure resulting 
    from this one-time surveillance extension is low. No changes are 
    being made to any accident initiator. No analyzed accident scenario 
    is being changed. The initiating conditions and assumptions of 
    previously analyzed accidents remain unchanged. Therefore, the 
    proposed change does not involve a significant increase in the 
    probability of a previously evaluated accident.
        This change does not involve a physical change to the plant and 
    does not affect the acceptance criteria specified in the TS for 
    snubber functional testing, nor does this change reduce the remedial 
    actions required for inoperable snubbers. Therefore, the proposed 
    change does not involve a significant increase in the consequences 
    of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed amendment does not involve any physical changes to 
    the plant or the modes of plant operation defined in Appendix A of 
    the operating license. The proposed amendment does not involve the 
    addition or modification of plant equipment nor does it alter the 
    design or operation of any plant systems. The one-time surveillance 
    interval extension proposed by this change will not reduce the 
    capability of the snubbers to perform their design function.
        Therefore, operation of the facility in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The margin of safety depends on the maintenance of specific 
    operating parameters
    
    [[Page 62712]]
    
    and systems within design requirements and safety analysis 
    assumptions.
        The proposed amendment does not involve revisions to any safety 
    limits or safety system setting that would adversely impact plant 
    safety. The proposed amendment does not affect the ability of 
    systems, structures or components important to the mitigation and 
    control of design bases accident conditions within the facility. In 
    addition, the proposed amendment does not affect the ability of 
    safety systems to ensure that the facility can be maintained in a 
    shutdown or refueling condition for extended periods of time, and 
    sufficient instrumentation and control capability is available for 
    monitoring and maintaining the unit status.
        The proposed change is for a one-time extension to the 
    surveillance interval for functional testing of snubbers specified 
    in Technical Specification 4.7.12.d. The proposed change continues 
    to adequately limit plant operation between required snubber 
    surveillances by ensuring the required surveillances are performed 
    by November 30, 2000. Therefore, the proposed change continues to 
    limit snubber wear due to vibration and elevated temperatures. The 
    elevated temperatures and vibration experienced during plant 
    operation are the primary contributors to snubber wear.
        In addition, snubber-testing experience has shown that the 
    historical failure rate of snubbers is low. There have been seven 
    refueling outages since Unit 2's startup in 1987. Only during the 
    first refueling outage, 2R01, did the snubber functional test sample 
    plan identify any inoperable snubbers. In that outage, seven 
    snubbers tested inoperable. All failed due to damage sustained 
    during original construction and startup activities. Since 2R01, no 
    inoperable snubbers were found by sample plan functional testing 
    performed during each surveillance interval. Also, the latest visual 
    inspections performed on the Unit 2 snubbers (during 2R07) revealed 
    no evidence of damage or potential problems with any snubber.
        This change does not involve a physical change to the plant and 
    does not affect the acceptance criteria specified in the TS for 
    snubber functional testing, nor does this change reduce the remedial 
    actions required for inoperable snubbers. The snubbers and systems 
    supported by the snubbers will continue to be available to perform 
    their intended safety functions during the requested extension 
    period.
        Therefore, operation of the facility in accordance with the 
    proposed amendment will not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Sheri R. Peterson.
    
    Entergy Gulf States, Inc., and Entergy Operations, Inc., Docket No. 50-
    458, River Bend Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: July 30, 1999.
        Description of amendment request: The request proposes changes to 
    the Technical Specifications (TSs) and the operating license to extend 
    operation of the station from its licensed power of 2894 megawatts 
    thermal (MWt) to the uprated power level of 3039 MWt, an increase of 5 
    percent. The proposed changes are to (1) extend the definition of rated 
    thermal power in TS Section 1.1 and the operating license to 3039 MWt; 
    (2) reduce the thermal power safety limit of TSs 1.4, 2.1.1.1, 3.2.1, 
    3.2.2, 3.2.3, 3.3.1.1, 3.4.3, and 3.7.5; (3) increase the reactor steam 
    dome pressure in TS Table 3.1.4-1, TS 3.4.12, and SR 3.5.3.3; (4) 
    increase the control rod drive charging water header pressure in TSs 
    3.1.5, 3.9.5, and 3.10.8; (5) increase the standby liquid control (SLC) 
    system Boron-10 enrichment and concentration criteria in TS 3.1.7; (6) 
    increase the surveillance test discharge pressure for the SLC pump in 
    surveillance requirement (SR) 3.1.7.7; (7) increase the allowable value 
    of the reactor vessel steam dome pressure--high scram setpoint in TS 
    Table 3.3.1.1-1; (8) increase the allowable value for the anticipated 
    transient without scram--reactor pressure trip reactor steam dome 
    pressure--high setpoint in SR 3.3.4.2.4; (9) revise the safety, relief, 
    and low low set function of the main steam safety/relief valves (SRVs) 
    in SRs 3.3.6.4.3 and 3.4.4.1; (10) increase the upper and lower bounds 
    on reactor pressure for the purposes of performing reactor core 
    isolation cooling pump flow rate surveillance at high pressure in SR 
    3.5.3.3; (11) increase the main steam line flow--high reactor isolation 
    trip in TS Table 3.3.6.1-1; (12) reduce the thermal power limits for 
    single loop operation in TS 3.4.1; (13) increase the upper and lower 
    bounds on reactor pressure for the purposes of performing pressure 
    isolation valve surveillance at high pressure in SR 3.4.6.1; and (14) 
    revise the reactor coolant system pressure/temperature limits in TS 
    3.4.11 (including replacing TS Figure 3.4.11-1 with figures for 14 and 
    32 effective full power years of operation). Item (9) includes 
    increasing the main steam SRV setpoint tolerance from +0%, -2% to [plus 
    or minus] 3% in SR 3.4.4.1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Will the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The increase in power level discussed herein will not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        The probability (frequency of occurrence) of Design Basis 
    Accidents occurring is not affected by the increased power level, as 
    the regulatory criteria established for plant equipment (ASME 
    [American Society of Mechanical Engineers] Code, IEEE [Institute of 
    Electrical and Electronic Engineers] standards, NEMA [National 
    Equipment Manufacturers Association] standards, Reg[ulatory] Guide 
    criteria, etc.) will still be complied with at the uprated power 
    level. An evaluation of the BWR [boiling water reactor] 
    probabilistic risk assessments concludes that the calculated core 
    damage frequencies will not significantly change due to [the] power 
    uprate. Scram setpoints (equipment settings that initiate automatic 
    plant shutdowns) will be established such that there is no 
    significant increase in scram frequency due to [the] uprate. No new 
    challenges to safety-related equipment will result from [the] power 
    uprate.
        The changes in consequences of hypothetical accidents which 
    would occur from 102% of the uprated power, compared to those 
    previously evaluated from [greater than or equal to] 102% of the 
    original power, are in all cases insignificant, because the accident 
    evaluations from [the] power uprate to 105% of original power 
    ([approximately] 106% of original steam) flow will not result in 
    exceeding the NRC-approved acceptance [criteria] limits. The 
    spectrum of hypothetical accidents and transients has been 
    investigated, and are shown to meet the plant's currently licensed 
    regulatory criteria. In the area of core design, for example, the 
    fuel operating limits such as Maximum Average Planar Linear Heat 
    Generation Rate (MAPLHGR) and Safety Limit Minimum Critical Power 
    Ratio (SLMCPR) are still met at the uprated power level, and fuel 
    reload analyses will show plant transients meet the criteria 
    accepted by the NRC as specified in NEDO-24011, ``GESTAR II''. 
    Challenges to fuel or ECCS [emergency core cooling system] 
    performance are evaluated, and shown to still meet the criteria of 
    10 CFR 50.46 and Appendix K [to 10 CFR 50], (Section 4.3 above, and 
    Regulatory Guide 1.70 and USAR [Updated Safety Analysis Report] 
    Section 6.3).
        Challenges to the containment have been evaluated, and the 
    containment and its associated cooling systems will continue to meet 
    10 CFR 50 Appendix A [General Design Criteria] Criterion 38, Long 
    Term Cooling, and Criterion 50, Containment.
        Radiological release events (accidents) have been evaluated, and 
    shown to meet the guidelines of 10 CFR 100 (Regulatory Guide 1.70 & 
    USAR Chapter 15).
        (2) Will the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
    
    [[Page 62713]]
    
        As summarized below, this change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        Equipment that could be affected by [the] power uprate has been 
    evaluated. No new operating mode, safety-related equipment lineup, 
    accident scenario, or equipment failure mode was identified. The 
    full spectrum of accident considerations defined in Regulatory Guide 
    1.70 have been evaluated and no new or different kind of accident 
    has been identified. [The power] Uprate uses already developed 
    technology, and applies it within the capabilities of already 
    existing plant equipment in accordance with presently existing 
    regulatory criteria to include NRC approved codes, standards, and 
    methods. GE [General Electric] has designed BWRs of higher power 
    levels than the uprated power of any of the currently operating BWR 
    fleet and no new power dependent accidents have been identified.
        The Technical Specification changes needed to implement [the] 
    power uprate require some small adjustments, but no change to the 
    plant's physical configuration. All changes have been evaluated, and 
    are acceptable.
        (3) Will the change involve a significant reduction in a margin 
    of safety?
        The calculated loads on all affected structures, systems and 
    components will remain within their design allowables for all design 
    basis event categories. No NRC acceptance criteria will be exceeded. 
    Only some design and operational margins are affected by [the] power 
    uprate. The margins of safety originally designed into the plant are 
    not affected by [the] power uprate. Because the plant configuration 
    and reactions to transients and hypothetical accidents will not 
    result in exceeding the presently approved NRC acceptance limits, 
    [the] power uprate can not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied for the power uprate.
        Although not required for the power uprate, the licensee also 
    requested a change to technical specifications to increase the main 
    steam SRV setpoint tolerance from +0%, -2% to [plus or minus] 3%. 
    However, the licensee's no significant hazards consideration for the 
    power uprate does not expressly address the change to the SRV setpoint 
    tolerance. Therefore, the NRC staff's review of this change is 
    presented below:
        (1) Will the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The main steam SRV's safety function lift setpoints are tested in 
    accordance with ASME Code requirements and the licensee's inservice 
    testing program. The setpoint tolerance determines whether the SRV 
    passes or fails the surveillance requirement and if additional valves 
    are to be tested. Notwithstanding the results of the safety function 
    lift setpoint test, if the measured value is outside a tolerance of 
    [plus or minus] 1%, the valve is reset to within [plus or minus] 1% of 
    the design lift setpoint. Therefore, the change to the SRV setpoint 
    tolerance does not affect the performance of any structure, system, or 
    component in the plant and does not affect the operation of the plant. 
    Accordingly, the change will not significantly increase the probability 
    or consequences of an accident previously evaluated.
        (2) Will the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The setpoint tolerance change does not alter the function of the 
    valves' over-pressure protection features, and the release of steam/
    water through the SRVs is addressed in previously evaluated accident 
    analysis. Therefore, the change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        (3) Will the changes involve a significant reduction in a margin of 
    safety?
        The change only affects whether a SRV passes or fails its safety 
    function surveillance requirement, as well as the total number of 
    valves to be tested. Regardless the outcome of these tests, all valves 
    tested will be returned to within [plus or minus] 1% of the design lift 
    setpoint. The 2% nominal ``as-left'' tolerance span is effectively the 
    same tolerance span as specified in the current technical 
    specifications. As a result, there is no significant reduction in a 
    margin of safety.
        Therefore, based on its review, it appears that the three standards 
    of 10 CFR 50.92(c) are satisfied, and the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, NW., Washington, DC 20005.
        NRC Section Chief: Robert A. Gramm.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: March 3, 1999.
        Description of amendment request: Entergy Operations, Inc. 
    (licensee) has proposed to revise Final Safety Analysis Report (FSAR) 
    Section 9.5.4.1, ``Diesel Generator Fuel Oil Storage and Transfer 
    Systems.'' The revision will change this section of the FSAR to 
    explicitly list the Waterford Steam Electric Station, Unit 3 (Waterford 
    3) deviations from the guidance described in American National 
    Standards Institute (ANSI) N195-1976, ``Fuel Oil Storage System for 
    Standby Diesel Generator.'' The licensee determined that these proposed 
    changes require Nuclear Regulatory Commission staff approval prior to 
    implementation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The proposed change revises the Waterford 3 FSAR to match the 
    current design of the Waterford 3 fuel oil storage and transfer 
    system. The change effectively requests deviations from portions of 
    ANSI N195-1976. None of these changes significantly increases the 
    probability of an accident because the Emergency Diesel Generator 
    (EDG) fuel oil system is not an initiator of any analyzed event. 
    There are no accidents analyzed in the Final Safety Analysis Report 
    (FSAR) that are initiated by the systems or components affected by 
    these changes.
        The deviation from ANSI N195-1976, which allows less than the 
    ANSI Standard recommended volume to be stored in the existing EDG 
    Fuel Oil Storage Tanks (FOSTs) A and B, will not significantly 
    increase the consequences of an accident. Waterford 3 contains at 
    least seven days of fuel oil in each FOST. Although the Waterford 3 
    FOSTs do not contain a 10% margin, there are numerous diesel fuel 
    oil vendors nearby from which to obtain fuel oil. Waterford 3 also 
    has the capability to transport EDG fuel oil from vendors by tanker 
    truck, train, or barge. This situation ensures that Waterford 3 will 
    have fuel oil readily available when there is a need for 
    replenishment. Waterford 3 does not store the additional amount of 
    fuel oil required for testing. A previous Technical Specification 
    (TS) Amendment addressed the Waterford 3 FOSTs not containing enough 
    fuel oil for testing. However, an exception to this requirement was 
    previously approved in TS Amendment 92.
        The request for deviation from the ANSI N195-1976 requirement 
    for the feed tank suction to be from above the bottom, will not 
    increase the consequences of any accident. Previous operating 
    experience at Waterford 3 has shown that since initial startup there 
    have not been any water or filter blockage problems attributed to 
    the bottom suction from the feed tank. The fuel oil in each feed 
    tank is replenished every 31 days during the EDG monthly 
    Surveillance Requirement (SR). Blockage problems are further 
    minimized because testing the FOSTs for particulates is performed 
    with a more conservative filter size than installed on the EDG 
    engine (0.8
    
    [[Page 62714]]
    
    microns versus 5 microns). Also, TS Surveillances require water and 
    sediment content to be verified and if water is present, for it to 
    be removed.
        The request for deviation from the ANSI N195-1976 requirement 
    for the feed tank overflow to discharge to the FOST will not 
    increase the consequences of any accident. The feed tank is equipped 
    with design features to ensure fuel oil is not depleted due to over-
    filling the feed tank. The feed tank contains a high level switch 
    that stops the transfer pump upon indication of high level and a 
    high level alarm that alerts the Control Room of high level in the 
    tank. A failure of both the feed tank high level switch and high 
    level alarm occurring simultaneously is very remote. These measures 
    will not prevent the loss of some fuel oil; however, two failures 
    would have to occur to prevent the Control Room from being notified. 
    Even if one EDG FOST were depleted because of the above failures, 
    the other EDG FOST would be available to ensure seven days of fuel 
    oil for one EDG.
        The request for deviation from the ANSI N195-1976 requirement to 
    have one pressure indicator located in the discharge of the fuel oil 
    transfer pump will not increase the consequences of any accident. A 
    pressure indicator on the discharge of the transfer pump could 
    indicate performance degradation of the pump; however, the Waterford 
    3 transfer pumps are designed for automatic operation. If a failure 
    of the transfer pump occurred, indication would appear in the 
    Control Room via the alarm for low feed tank level. The alarm for 
    low feed tank level is adequate to alert the Control Room of a 
    transfer pump malfunction. If a transfer pump were to malfunction, 
    the other transfer pump would be available to deliver fuel oil to 
    operate one EDG for at least seven days. ASME Section XI testing is 
    performed on the transfer pump once per quarter (temporary pressure 
    instrumentation is installed on the discharge of the pump to measure 
    pump differential pressure) to verify that pump performance has not 
    degraded. In addition, the transfer pumps are functionally tested 
    every month during routine testing of the EDGs.
        The requested deviations from ANSI N195-1976 do not affect the 
    consequences of an accident because none of the requested deviations 
    will prevent the EDG from having seven days of fuel oil available 
    (without multiple failures). Therefore, the EDG fuel oil system will 
    perform as required to provide sufficient fuel oil to the EDG to 
    mitigate the consequences of design basis accidents.
        Therefore, based on all the above, the proposed changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        The proposed change revises the Waterford 3 FSAR to match the 
    current design of the Waterford 3 fuel oil storage and transfer 
    system. This change is a change to a commitment, and has no [a]ffect 
    on the current diesel fuel oil storage system or how it is operated, 
    nor does it [a]ffect any other safety systems or components, or the 
    way the plant is operated. The change does not affect any accident 
    analysis assumptions (including a loss of offsite power) or accident 
    analysis conclusions. Therefore, the proposed change will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No
        The proposed change revises the Waterford 3 FSAR to match the 
    current design of the Waterford 3 fuel oil storage system. Although 
    Waterford 3 deviates from certain ANSI N195-1976 requirements, these 
    deviations do not result in any changes to the fuel oil storage 
    system or accident analyses. The deviations do not affect the 
    ability of any safety systems required to protect the multiple 
    barriers. No accident mitigatiors are affected by the change because 
    the amount of available fuel oil has not changed. As a result, the 
    proposed deviations will not cause a significant decrease in the 
    margin of safety or prevent Waterford 3 from safely shutting down. 
    The result of using Probabilistic Safety Assessment techniques 
    conclude that increasing the fuel oil storage capacity at Waterford 
    3 to comply with the ANSI requirements has no risk significance. The 
    specific [a]ffects of the deviations on the margin of safety are 
    addressed below.
        The current TS for stored EDG fuel oil ensures there is 
    sufficient fuel oil to operate one EDG for seven days assuming the 
    worst case single active or passive failure. Fuel oil is readily 
    available due to the number of vendors in the vicinity of Waterford 
    3. Waterford 3 is also capable of replenishing EDG fuel oil via 
    tanker truck, train, or barge. Therefore, this change does not 
    affect the supply of EDG fuel oil being maintained at Waterford 3. 
    This supply of fuel oil is sufficient to power the ESF systems 
    required to mitigate design basis accidents. A previous TS Amendment 
    addressed the Waterford 3 FOSTs not containing enough fuel oil for 
    testing.
        The current feed tank design with the suction from the bottom 
    instead of on the side as required by ANSI N195-1976 will not 
    significantly decrease the margin of safety. Waterford 3 has not 
    experienced particulate or water accumulation in the feed tanks. The 
    fuel oil in the tank is essentially turned-over every 31 days during 
    the EDG monthly SR, and TS Surveillances ensure water and sediment 
    content are verified. Additionally, particulate testing is performed 
    on the EDG FOSTs using a test filter with a smaller micron size than 
    is on the engine. This will assure the EDG engine is not subject to 
    failures due to particulate or water accumulation in the feed tanks.
        The request for deviation from the ANSI N195-1976 requirement 
    for the feed tank overflow to discharge to the FOST will not 
    significantly decrease the margin of safety. The feed tank is 
    equipped with two safety measures that would have to fail in order 
    to allow a loss of EDG fuel oil due to over-filling a feed tank. A 
    failure of these safety measures (high level switch to stop the 
    transfer pump and a high level alarm in the feed tank) occurring 
    simultaneously is very remote.
        The request for deviation from ANSI N195-1976 to have one 
    pressure indicator located at the discharge of the fuel oil transfer 
    pump will not significantly decrease the margin of safety. A 
    pressure indicator on the discharge of the transfer pump could 
    indicate performance degradation of the pump. If a failure of the 
    transfer pump occurred, indication would appear in the Control Room 
    via the alarm for low feed tank level. The alarm for low feed tank 
    is adequate to alert the control room of a transfer pump 
    malfunction. However, if the transfer pump were to malfunction, the 
    other transfer pump would be available to deliver fuel oil to 
    operate one EDG for at least seven days. ASME Section XI testing is 
    performed on the transfer pump once per quarter (temporary pressure 
    instrumentation is installed on the discharge of the pump to measure 
    pump differential pressure) to verify that pump performance has not 
    degraded. In addition, the transfer pumps are functionally tested 
    every month during routine testing of the EDGs.
        Therefore, based on all the above, the proposed changes will not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: N.S. Reynolds, Esquire, Winston & Strawn 
    1400 L Street NW., Washington, DC 20005-3502.
        NRC Section Chief: Robert A. Gramm.
    
    PECO Energy Company, Docket Nos. 50-352 and 50-353, Limerick Generating 
    Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of amendment request: September 27, 1999.
        Description of amendment request: The proposed change to the 
    Technical Specifications (TSs), if approved, will clarify several 
    administrative requirements, delete redundant requirements, and correct 
    typographical errors. These revisions affect TS Sections 3.8.3.1, 
    3.8.3.2, 6.2.2, 6.5.1.2, 6.8.2, 6.9.1.5, and 6.9.1.6.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed TS changes do not involve a significant increase 
    in the probability or
    
    [[Page 62715]]
    
    consequences of an accident previously evaluated.
        The changes are administrative in nature and do not impact the 
    operation, physical configuration, or function of plant equipment or 
    systems. The changes do not impact the initiators or assumptions of 
    analyzed events, nor do they impact mitigation of accidents or 
    transient events. Therefore, these changes do not increase the 
    probability of occurrence or consequences of an accident previously 
    evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are administrative in nature and do not 
    alter plant configuration, require that new equipment be installed, 
    alter assumptions made about accidents previously evaluated, or 
    impact the operation or function of plant equipment. Therefore, 
    these changes do not create the possibility of a new or different 
    kind of accident than previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The proposed changes are administrative in nature and do not 
    involve any physical changes to plant structures, systems, or 
    components (SSCs), or the manner in which these SSCs are operated, 
    maintained, modified, tested, or inspected. The proposed changes do 
    not involve a change to any safety limits, limiting safety system 
    settings, limiting conditions of operation, or design parameters for 
    any SSC. The proposed changes do not impact any safety analysis 
    assumptions and do not involve a change in initial conditions, 
    system response times, or other parameters affecting any accident 
    analysis. Therefore, these changes do not involve any reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: J.W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101.
        NRC Section Chief: James W. Clifford.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch 
    Nuclear Plant, Units 1 and 2, Appling County, Georgia
    
        Date of amendment request: October 1, 1999.
        Description of amendment request: The proposed amendments would 
    revise the minimum fuel oil level for the diesel generator day tanks in 
    Surveillance Requirement 3.8.1.3 and would change the acceptable fuel 
    oil level storage band in Required Action Statement B of Limiting 
    Condition for Operation 3.8.3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The diesel generators are designed to supply power to the 
    emergency systems needed to mitigate the consequences of design 
    basis accidents such as LOCA/LOSP [loss-of-coolant accident/loss-of-
    offsite power]. They (the diesel generators) do not function to 
    prevent accidents. Reducing the level requirement in the day tanks 
    and raising the level requirement in the fuel oil storage tanks will 
    therefore not increase the probability of occurrence of a LOCA/LOSP 
    event. Furthermore, this proposed change does not affect any other 
    system or piece of equipment designed to prevent the occurrence of 
    any other design basis accident or transient. Therefore, reducing 
    the required level in the day tanks and raising the level in the 
    fuel oil storage tanks will not increase the probability of 
    occurrence of any previously evaluated accident or transient.
        The consequences of previously evaluated events will not be 
    significantly increased because, with the 500-gallon day tank 
    requirement and the increased storage tank supply, ample fuel will 
    be available to supply the diesel generators for the duration of a 
    LOCA/LOSP event or a station blackout event. Therefore, the 
    consequences of an accident previously evaluated are not increased 
    by this modification.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        Lowering TS SR 3.8.1.3 from [greater than or equal to] 900 
    gallons to [greater than or equal to] 500 gallons and raising TS SR 
    3.8.3.1 from [greater than or equal to] 33,000 gallons to [greater 
    than or equal to] 33,320 gallons will have no impact on the normal 
    or emergency operation of the diesel generator and its support 
    systems. For example, diesel generator transfer pumps and supply 
    tank transfer pumps will continue to perform as necessary to insure 
    an adequate supply in the respective tanks for accident mitigation.
        As a result, since no new unanalyzed modes of operation are 
    introduced, the possibility of a new or different type of accident, 
    from any previously evaluated is not introduced.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        The Bases for TS SR 3.8.1.3 states that the day tank must carry 
    enough fuel oil to provide for one hour of operation, plus a 10 
    percent margin. This requirement is based on ANSI N195-1976 (Section 
    6.1).
        The present 900-gallon requirement in the present Technical 
    Specifications provides for 3.5 hours of continuous operation. 
    Reducing the volume requirement to 500 gallons will continue to 
    provide ample margin above the 1-hour requirement. In fact, 500 
    gallons in the day tank provides for 1.89 hours of continuous 
    operation.
        The Bases for TS SR 3.8.3.1 states that the fuel in the storage 
    tanks (33,000 gallons) alone is sufficient to account for seven days 
    of continuous operation. This is true for 33,000 gallons of usable 
    fuel. However, each storage tank contains approximately 1,438 
    gallons of unusable fuel. Additionally, part of the current design 
    bases for the emergency diesel generators is the ability to run four 
    of the five diesels continuously for seven days at a load of 3250 
    kW. With 500 gallons in each of the four diesel's day tanks and 
    33,320 gallons in each of the five storage tanks, the system is 
    capable of running continuously for 7 days. Ample onsite fuel 
    capacity remains to operate the diesels continuously for a longer 
    period than required to replenish the supply from outside sources. 
    For the above reasons, the margin of safety is not significantly 
    reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC.
        NRC Section Chief: Richard L. Emch, Jr.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia, Docket No. 50-321, Edwin I. Hatch Nuclear 
    Plant, Unit 1, Appling County, Georgia
    
        Date of amendment request: October 15, 1999.
        Description of amendment request: The proposed amendment would 
    change the Safety Limit Minimum Critical Power Ratios (SLMCPR) in 
    Technical Specification (TS) 2.1.1.2 to reflect results of a cycle-
    specific calculation performed for Unit 1 Operating Cycle 19. The 
    calculation was done using the new NRC-approved methodology for 
    determining SLMCPRs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed Technical Specification changes do not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The derivation of the revised SLMCPRs for Plant Hatch Unit 1 
    Cycle 19 for incorporation
    
    [[Page 62716]]
    
    into the TS, and their use to determine cycle-specific thermal 
    limits, have been performed using NRC-approved methods and 
    procedures. The procedures incorporate cycle-specific parameters and 
    reduced power distribution uncertainties in the determination of the 
    lower value for SLMCPRs. These calculations do not change the method 
    of operating the plant and have no effect on the probability of an 
    accident initiating event or transient.
        The basis of the MCPR Safety Limit is to ensure no mechanistic 
    fuel damage is calculated to occur if the limit is not violated. The 
    new SLMCPRs preserve the existing margin to transition boiling and 
    the probability of fuel damage is not increased. Therefore, the 
    proposed changes do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes result only from a revised method of 
    analysis for the Unit 1 Cycle 19 core reload. These changes do not 
    involve any new method for operating the facility and do not involve 
    any facility modifications. No new initiating events or transients 
    result from these changes. Therefore, the proposed TS changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety as defined in the TS bases will remain the 
    same. The new SLMCPRs are calculated using NRC-approved methods and 
    procedures which are in accordance with the current fuel design and 
    licensing criteria. The SLMCPRs remain high enough to ensure that 
    greater than 99.9% of all fuel rods in the core are expected to 
    avoid transition boiling if the limit is not violated, thereby 
    preserving the fuel cladding integrity.
        Therefore, the proposed TS changes do not involve a reduction in 
    the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC.
        NRC Section Chief: Richard L. Emch, Jr.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia, Docket No. 50-366, Edwin I. Hatch Nuclear 
    Plant, Unit 2, Appling County, Georgia.
    
        Date of amendment request: October 15, 1999.
        Description of amendment request: The proposed amendment would 
    change the Safety Limit Minimum Critical Power Ratios (SLMCPR) in 
    Technical Specification (TS) 2.1.1.2 to reflect results of a cycle-
    specific calculation performed for Unit 2 Operating Cycle 16. The 
    calculation was performed using the new NRC-approved methodology for 
    determining SLMCPRs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed Technical Specification changes do not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The derivation of the revised SLMCPRs for Plant Hatch Unit 2 
    Cycle 16 for incorporation into the TS, and their use to determine 
    cycle-specific thermal limits, have been performed using NRC-
    approved methods and procedures. The procedures incorporate cycle-
    specific parameters and reduced power distribution uncertainties in 
    the determination of the lower value for SLMCPRs. These calculations 
    do not change the method of operating the plant and have no effect 
    on the probability of an accident initiating event or transient.
        The basis of the MCPR Safety Limit is to ensure no mechanistic 
    fuel damage is calculated to occur if the limit is not violated. The 
    new SLMCPRs preserve the existing margin to transition boiling and 
    the probability of fuel damage is not increased. Therefore, the 
    proposed changes do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes result only from a revised method of 
    analysis for the Unit 2 Cycle 16 core reload. These changes do not 
    involve any new method for operating the facility and do not involve 
    any facility modifications. No new initiating events or transients 
    result from these changes. Therefore, the proposed TS changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety as defined in the TS bases will remain the 
    same. The new SLMCPRs are calculated using NRC-approved methods and 
    procedures which are in accordance with the current fuel design and 
    licensing criteria. The SLMCPRs remain high enough to ensure that 
    greater than 99.9% of all fuel rods in the core are expected to 
    avoid transition boiling if the limit is not violated, thereby 
    preserving the fuel cladding integrity.
        Therefore, the proposed TS changes do not involve a reduction in 
    the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC.
        NRC Section Chief: Richard L. Emch, Jr.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: October 18, 1999.
        Description of amendment request: The proposed amendment would 
    revise the activated charcoal testing methodology in accordance with 
    the guidance provided in NRC Generic Letter 99-02, ``Laboratory Testing 
    of Nuclear Grade Activated Charcoal.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Will the proposed changes involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        The Standby Gas Treatment (SBGT) system is used to support 
    mitigation of the consequences of postulated accidents. The SBGT 
    system is not considered an initiator of any analyzed accident. 
    There is no change in function or operation of the system. The 
    proposed change only revises the charcoal laboratory testing 
    protocol to a more current standard that is more reliable, accurate 
    and conservative. The change in relative humidity proposed is 
    likewise in accordance with accepted guidance and reflective of the 
    Vermont Yankee system configuration, which utilizes heaters to 
    reduce the incoming humidity. The change in iodide removal 
    efficiency is also more conservative.
        Thus, the probability or consequences of previously analyzed 
    accidents is not significantly increased.
        2. Will the proposed changes create the possibility of a new or 
    different kind of accident from any previously evaluated?
    
    [[Page 62717]]
    
        This change does not affect the design or mode of operation of 
    any plant system, structure or component. No physical alteration of 
    plant structures, systems or components is involved and no new or 
    different equipment will be installed. The proposed change only 
    modifies the laboratory testing protocol and acceptance criteria to 
    a more currently accepted standard.
        Thus, the proposed change does not create the possibility of a 
    new or different [kind of] accident from those previously evaluated.
        3. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not involve a 
    significant reduction in a margin of safety.
        The proposed changes in laboratory test protocol do not 
    adversely affect the operation of any systems, structures or 
    components. In fact, adopting the newer test standard will provide 
    greater assurance that the charcoal will perform its intended 
    function of accident consequence mitigation.
        Thus, the proposed change does not significantly reduce a margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Section Chief: James W. Clifford.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: October 21, 1999.
        Description of amendment request: The proposed amendment makes 
    editorial and administrative changes to the Technical Specifications 
    (TSs) by correcting two administrative errors and changing the 
    designation of a TS-referenced figure. These changes do not materially 
    change the meaning or application of any TS requirement.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Will the proposed changes involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        The proposed changes are administrative or editorial in nature 
    and do not involve any physical changes to the plant. The 
    administrative changes do not materially affect any existing 
    technical requirement and do not reduce the actions that are 
    currently taken to ensure operability of plant structures, systems 
    or components.
        The changes correct past administrative errors and change a 
    reference in the Technical Specifications and do not revise the 
    methods of plant operation which could increase the probability or 
    consequences of previously evaluated accidents. No new modes of 
    operation are introduced by the proposed changes such that a 
    previously evaluated accident is more likely to occur or more 
    adverse consequences would result.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Will the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        These changes are administrative in nature and do not affect the 
    operation of any systems or components, nor do they involve any 
    potential initiating events that would create any new or different 
    kind of accident. There are no changes to the design assumptions, 
    conditions, configuration of the facility, or the manner in which 
    the plant is operated and maintained.
        The changes do not affect assumptions contained in plant safety 
    analyses or the physical design and/or modes of plant operation. 
    Consequently, no new failure mode is introduced due to the 
    administrative changes.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated for Vermont Yankee.
        3. Will the proposed changes involve a significant reduction in 
    a margin of safety?
        There are no changes being made to the Technical Specification 
    safety limits or safety system settings. The operating limits and 
    functional capabilities of systems, structures, and components are 
    unchanged as a result of these administrative changes. These 
    proposed changes do not affect any equipment involved in potential 
    initiating events or safety limits. There is no change to the basis 
    for any Technical Specification that is related to the establishment 
    of, or the maintenance of, a nuclear safety margin.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Section Chief: James W. Clifford.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant (PBNP), Units 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendment request: October 5, 1999.
        Description of amendment request: The proposed amendments would 
    make changes to the Technical Specifications (TSs) that are necessary 
    to eliminate inconsistencies in the TSs pertaining to decay heat 
    removal requirements (TSs 15.3.1.A.3, 15.3.3.A, and 15.3.3.C). An 
    additional change to the requirements in TS 15.3.1.A.4 for pressurizer 
    safety valve operability is also proposed to provide appropriate 
    coordination with low temperature overpressure protection requirements. 
    Bases revisions are provided consistent with the proposed amendments 
    and to administratively correct references related to accumulator 
    operability in the Bases for TS 15.3.3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Technical Specifications 15.3.1.A.3, 15.3.3.A.3 and 15.3.3.C are 
    all interrelated in that they each provide direction for required 
    decay heat removal capability, either directly or indirectly by 
    providing requirements for both support and supported systems. TS 
    15.3.1.A.3 provides requirements for the operation of the reactor 
    coolant system loops, steam generators, reactor coolant pumps and 
    residual heat removal loops as necessary to support decay heat 
    removal from a shutdown unit. TS 15.3.3.A provides requirements for 
    operation of the high head safety injection and low head residual 
    heat removal system. Specifically, TS 15.3.3.A.3 provides 
    requirements for inoperability of the residual heat removal system 
    which accounts for the dual purpose of injection and decay heat 
    removal. TS 15.3.3.C.2 provides requirements for operation of the 
    Component Cooling Water System, a primary support system for both 
    Residual Heat Removal System and Reactor Coolant Pump operation. The 
    proposed Specifications require redundancy of decay heat removal and 
    require placing the plant in a safe condition, maximizing the 
    availability of decay heat removal methods when redundancy is lost. 
    Appropriate allowances and actions are required to ensure uniform 
    mixing of boron for reactivity control with the unit shutdown and 
    provide for appropriate allowances to facilitate surveillance 
    testing, and refueling operations. The time limits placed on all 
    actions are consistent with safe operations, industry and NRC 
    guidance. Therefore the probability of a
    
    [[Page 62718]]
    
    loss of shutdown cooling or loss of subcooling; or a loss of 
    shutdown reactivity control is minimized.
        Amendments are also proposed to provide for coordination of 
    Pressurizer Safety Valve and Pressurizer Power Operated Relief Valve 
    operability requirements to ensure redundant overpressure protection 
    is provided for all operating conditions. Proposed actions for 
    inoperability of Pressurizer Safety Valves minimizes the time in 
    that condition. Operation of the valves is not changed. Thus, the 
    probability of a loss of coolant due to inadvertent opening of the 
    valves is not increased. In addition, overpressure protection is 
    maintained under all conditions such that the probability of an 
    overpressure due to an analyzed event is not increased.
        The proposed changes do not affect potential leakage paths for 
    radiation to the environment, or of key safety barriers, and ensure 
    appropriate system and function redundancy is maintained. Therefore 
    the consequences of an accident previously evaluated will not 
    increase.
        Therefore, operation of the Point Beach Nuclear Plant in 
    accordance with the proposed amendments does not result in a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed amendments do not alter the operation or method of 
    function of the Residual Heat Removal System, Component Cooling 
    Water System, Pressurizer Safety Valves, or Power Operated Relief 
    Valves. The amendments provide for consistency of decay heat removal 
    and pressure relief requirements within the Specifications providing 
    assurance these functions can be maintained during all required 
    plant conditions. Operations are not altered in any way that could 
    introduce a new accident initiator not previously considered in the 
    PBNP Safety Analyses. Therefore, operation of the Point Beach 
    Nuclear Plant in accordance with the proposed amendments cannot 
    create the possibility of a new or different kind of accident than 
    any previously evaluated.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not result in a significant reduction 
    in a margin of safety.
        The proposed amendments ensure redundancy of the decay heat 
    removal and overpressure protection over the complete range of 
    operating conditions. Limitations are provided to ensure timely 
    action to restore the functions to an operable condition consistent 
    with their importance to safety. Appropriate allowances and actions 
    are required to ensure uniform mixing of boron for reactivity 
    control with the unit shutdown and provide for appropriate 
    allowances to facilitate surveillance testing, and refueling 
    operations consistent with overall safety. The functions or method 
    of function of the systems or components affected are not being 
    altered. Therefore, operation of the Point Beach Nuclear Plant in 
    accordance with the proposed amendments cannot result in a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Claudia M. Craig.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: October 21, 1999.
        Description of amendment request: The request proposes to revise 
    Technical Specification (TS) 3.4.10, Pressurizer Safety Valves (PSV), 
    of the improved Technical Specifications issued March 31, 1999. The 
    proposed revision is to reduce the safety valve set pressure in 
    Limiting Condition for Operation (LCO) 3.4.10, and increase the 
    setpoint tolerance in Surveillance Requirement (SR) 3.4.10.1. The PSV 
    setpoint and setpoint tolerance is proposed to be changed from 2485 
    psig plus or minus 1% to 2460 psig plus or minus 2% in the LCO. The 
    tolerance of plus or minus 1% in the SR is for resetting the setpoint 
    after testing, if this is needed. The licensee also submitted the Bases 
    pages for TS 3.4.10, which show modifications to reflect the changes to 
    the TSs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Any evaluations performed on an overpressure transient 
    conservatively assume the upper limit of the pressurizer safety 
    valve (PSV) tolerance as the pressure to which the reactor coolant 
    system (RCS) is subjected. The proposed change to the lower 
    tolerance limit of the pressure set point means that an overpressure 
    transient may be terminated at a pressure that is lower than assumed 
    in the analysis. It has also been determined that the design 
    transients are not adversely affected because the limiting 
    transients are not sensitive to the pressure tolerance decrease. 
    Therefore, the primary system pressure boundary is not challenged by 
    the PSV lower tolerance limit change. The change in the upper limit 
    of the PSV tolerance does not challenge the upper limit of the 
    overpressure protection. The maximum opening set pressure is not 
    changed, and therefore, does not impact analyses performed for 
    overpressure transients. Although the lower PSV set point would 
    result in a lower qualified valve flow rate, the slightly lower 
    valve flow rate would be more than compensated for by the reduced 
    valve opening pressure. The change to the PSV set point and set 
    point tolerance does not change the conclusions of the existing 
    thermal hydraulic analysis for the pressurizer safety and relief 
    system. The design function of the valves is not being changed. 
    Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated in the USAR [Wolf Creek Updated Safety Analysis 
    Report].
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change would allow the PSV minimum actuation 
    pressure to be as low as 2411 psig. The pressurizer power-operated 
    relief valve (PORV) actuation set point is 2335 psig. Therefore, the 
    margin between the PORV and PSV actuation set points could be as low 
    as 76 psi, which is a reduction of 49 psi from the current 125 psi 
    margin. Even with the 30 psi pressure control uncertainty, the 
    actuation set point margin of 76 psi is considered adequate and the 
    PORVs are expected to continue to actuate before the PSVs during 
    Condition 1 transients. As such, the proposed change will not have 
    any adverse effect on the control systems. Except for the reduced 
    lower set point, the design and operation of the PSVs are not being 
    changed. The maximum opening pressure is not being changed. The only 
    effect of this change would be that the PSVs could open at a lower 
    pressure, but still above the PORV actuation set point. Therefore, 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated is not created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The PSVs provide, in conjunction with the reactor protection 
    system, overpressure protection for the RCS. The PSVs are designed 
    to prevent the system pressure from exceeding the system safety 
    limit, 2735 psig, which is 110% of the design pressure. The change 
    in the upper limit of the PSV tolerance from plus or minus 1% to 
    plus or minus 2% with a reduction in the nominal set point from 2485 
    psig to 2460 psig does not challenge the upper limit of the 
    overpressure protection. The maximum opening pressure set point is 
    not changed, and therefore, does not impact analyses performed for 
    overpressure transients. The change to PSV set point and set point 
    tolerance does not change the conclusions of the existing thermal 
    hydraulic analysis for the pressurizer safety and relief system. For 
    all non-LOCA [non-loss of coolant accident] events the analyses 
    support the change in PSV set point and set point tolerance from 
    2485 psig plus or minus 1% to 2460 psig plus or minus 2%. The change 
    in the PSV set
    
    [[Page 62719]]
    
    point and set point tolerance also has no effect on the Reactor 
    Protection or Engineered Safety Features Systems trip set points. 
    Thus, the proposed change does not involve a significant reduction 
    in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Section Chief: Stephen Dembek.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Indiana Michigan Power Company, Docket No. 50-315 and 50-316, Donald C. 
    Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of amendment request: September 23, 1999, as supplemented 
    October 11, 1999.
        Brief description of amendment request: The proposed amendments 
    involve movement of loads in excess of the design-basis seismic 
    capability of the auxiliary building load handling equipment and 
    structures. The proposed amendment requests approval to move the steam 
    generator sections through the auxiliary building and to disengage 
    crane travel interlocks, and also requests relief from performance of 
    Technical Specification Surveillance Requirement 4.9.7.1.
        Date of publication of individual notice in Federal Register: 
    October 26, 1999 (64 FR 57665).
        Expiration date of individual notice: November 26, 1999.
    
    Indiana Michigan Power Company, Docket No. 50-315 and 50-316, Donald C. 
    Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of amendment request: October 1, 1999.
        Brief description of amendment request: The proposed amendments 
    involve the resolution of an unreviewed safety question related to 
    certain small-break loss-of-coolant accident scenarios for which there 
    may not be sufficient containment recirculation sump water inventory to 
    support continued operation of the emergency core cooling system and 
    containment spray system pumps during and following switchover to cold 
    leg recirculation. Resolution of this issue consists of a combination 
    of physical plant modifications, new analyses of containment 
    recirculation sump inventory, and resultant changes to the accident 
    analyses to ensure sufficient water inventory in the containment 
    recirculation sump. In addition, the licensee proposes to change the 
    Technical Specifications dealing with the refueling water storage tank 
    inventory and temperature, the required amount of ice in each ice 
    basket in the containment, and the delay to start the containment air 
    recirculation/ hydrogen skimmer fans.
        Date of publication of individual notice in Federal Register: 
    October 29, 1999 (64 FR 58458).
        Expiration date of individual notice: November 29, 1999.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and electronically from the ADAMS Public 
    Library component on the NRC Web site, http://www.nrc.gov (the 
    Electronic Reading Room).
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: April 21, 1999, as supplemented 
    October 15, 1999.
        Brief description of amendment: The amendment allows for a one-time 
    extension of the reactor protection system and engineered safety 
    features actuation system instruments.
        Date of issuance: October 29, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 205.
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration (NSHC): Yes October 14, 1999 (64 FR 55777). The October 
    15, 1999, letter provided clarifying information that did not change 
    the initial proposed no significant hazards consideration. The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    NSHC determination. No comments have been received. The notice also 
    provided for an opportunity to request a hearing by October 28, 1999, 
    but indicated that if the Commission makes a final NSHC determination, 
    any such hearing would take place after issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final determination of NSHC are contained in 
    a Safety Evaluation dated October 29, 1999.
    
    [[Page 62720]]
    
        Attorney for licensee: Mr. Brent L. Brandenburg, Assistant General 
    Counsel, Consolidated Edison Company of New York, Inc., 4 Irving 
    Place--1822, New York, NY 10003.
        NRC Section Chief: Sheri Peterson.
    
    Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: August 4, 1999.
        Brief description of amendments: The amendments revise the TS 
    (Appendix A of the Catawba operating licenses) to: (1) modify Section 
    3.3.2 regarding the Nuclear Service Water System, and (2) Section 5.3.1 
    regarding operating personnel qualifications.
        Date of issuance: November 2, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 45 days from the date of issuance.
        Amendment Nos.: Unit 1-181; Unit 2-173.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 8, 1999 (64 
    FR 48861).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 2, 1999.
        No significant hazards consideration comments received: No
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio
    
        Date of application for amendment: October 22, 1997.
        Brief description of amendment: This amendment approves a proposed 
    modification that changes the Perry facility as described in the 
    Updated Safety Analysis Report. The change incorporates temperature 
    control valves and associated bypass lines around the Emergency Closed 
    Cooling system heat exchangers. These features are designed to ensure 
    operability of the Control Complex Chilled Water System under post-
    accident load conditions, without the need for compensatory measures.
        Date of issuance: October 29, 1999.
        Effective date: October 29, 1999.
        Amendment No.: 107.
        Facility Operating License No. NPF-58: This amendment authorizes 
    the revision of the Updated Safety Analysis Report.
        Date of initial notice in Federal Register: November 5, 1997 (62 FR 
    59922).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 29, 1999.
        No significant hazards consideration comments received: No
    
    Southern Nuclear Operating Company, Inc., et al., Docket Nos. 50-424 
    and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke 
    County, Georgia
    
        Date of application for amendments: May 18, 1999, as supplemented 
    by letter dated September 22, 1999.
        Brief description of amendments: The amendments revised 
    Surveillance Requirements (SR) 3.8.1.3 and 3.8.1.13 to reduce the 
    loading requirements for the emergency diesel generators (EDGs). 
    Revised SR 3.8.1.3 requires the EDGs be loaded and operated for 
    [greater than or equal to] 60 minutes at a load [greater than or equal 
    to] 6500 kW and [less than or equal to] 7000 kW at least every 31 days. 
    Revised SR 3.8.1.13 requires the EDGs to be loaded [greater than or 
    equal to] 6900kW and [less than or equal to] 7700 kW and operated as 
    close as practicable to 3390 kVA for 2 hours. For the remaining hours 
    of the test, the EDGs would be loaded [greater than or equal to] 6500 
    kW and [less than or equal to] 7000 kW and operated as close as 
    practicable to 3390 kVA.
        Date of issuance: October 25, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: Unit 1-109; Unit 2-87.
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 11, 1999 (64 FR 
    43780) The supplemental letter dated September 22, 1999, provided 
    clarifying information that did not change the scope of the May 18, 
    1999, application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 25, 1999.
        No significant hazards consideration comments received: No
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-280 and 50-
    281, Surry Power Station, Units 1 and 2, Surry County, Virginia
    
        Date of application for amendments: April 28, 1999.
        Brief Description of amendments: These amendments revise TS Section 
    3.4.A.4 for Units 1 and 2. The changes relax the minimum volume 
    requirement for the refueling water Chemical Addition Tank (CAT) from 
    4200 gallons to 3930 gallons. A minor administrative change is also 
    being made to TS Table 4.1-2B to correct an earlier printing error and 
    to delete a reference which no longer applies.
        Date of issuance: November 1, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: 222 and 222.
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    change the Technical Specifications.
        Date of initial notice in Federal Register: September 8, 1999 (64 
    FR 48869).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 1, 1999.
        No significant hazards consideration comments received: No
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a
    
    [[Page 62721]]
    
    reasonable opportunity for the public to comment, using its best 
    efforts to make available to the public means of communication for the 
    public to respond quickly, and in the case of telephone comments, the 
    comments have been recorded or transcribed as appropriate and the 
    licensee has been informed of the public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and 
    electronically from the ADAMS Public Library component on the NRC Web 
    site, http://www.nrc.gov (the Electronic Reading Room).
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By December 17, 1999, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and electronically from the ADAMS Public Library 
    component on the NRC Web site, http://www.nrc.gov (the Electronic 
    Reading Room). If a request for a hearing or petition for leave to 
    intervene is filed by the above date, the Commission or an Atomic 
    Safety and Licensing Board, designated by the Commission or by the 
    Chairman of the Atomic Safety and Licensing Board Panel, will rule on 
    the request and/or petition; and the Secretary or the designated Atomic 
    Safety and Licensing Board will issue a notice of a hearing or an 
    appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. A copy of the petition should also be sent
    
    [[Page 62722]]
    
    to the Office of the General Counsel, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, and to the attorney for the 
    licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: March 26, 1999, as supplemented 
    October 15, 1999.
        Brief description of amendment: The amendment allows for a one-time 
    extension of system functional tests. The test intervals are extended 
    for 37 months to coincide with the next refueling outage scheduled to 
    commence on June 3, 2000.
        Date of issuance: October 29, 1999.
        Effective date: As of the date of issuance to be implemented upon 
    receipt.
        Amendment No.: 204.
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Press release issued requesting comments as to proposed no 
    significant hazards consideration: Yes, October 22 and 24, 1999, 
    Peekskill Evening Star.
        The October 15, 1999, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration. The notice provided an opportunity to submit comments on 
    the Commission's proposed NSHC determination. No comments have been 
    received. The notice also provided for an opportunity to request a 
    hearing by October 28, 1999, but indicated that if the Commission makes 
    a final NSHC determination, any such hearing would take place after 
    issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final determination of NSHC are contained in 
    a Safety Evaluation dated October 29, 1999.
        Attorney for licensee: Mr. Brent L. Brandenburg, Assistant General 
    Counsel, Consolidated Edison Company of New York, Inc., 4 Irving 
    Place--1822, New York, NY 10003 NRC Section Chief: Sheri Peterson.
    
        Dated at Rockville, Maryland, this 9th day of November 1999.
    
        For the Nuclear Regulatory Commission.
    John A. Zwolinski,
    Director, Division of Licensing Project Management Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 99-29846 Filed 11-16-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
11/17/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-29846
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
62704-62722 (19 pages)
PDF File:
99-29846.pdf