96-29584. Biweekly Notice  

  • [Federal Register Volume 61, Number 224 (Tuesday, November 19, 1996)]
    [Notices]
    [Pages 58900-58910]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-29584]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from October 28, 1996, through November 7, 1996. 
    The last biweekly notice was published on November 6, 1996.
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By December 20, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first
    
    [[Page 58901]]
    
    prehearing conference scheduled in the proceeding, but such an amended 
    petition must satisfy the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: October 2, 1996
        Description of amendment request: The amendment would change 
    Figures 3.1.A-1, 3.1.A-2, and 3.1.A-3, Section 3.1.B and its Bases, 
    Figures 3.1.B-1 and 3.1.B-2, and the Bases of Section 4.3 and Figure 
    4.3-1 of the Technical Specifications by providing new pressure/
    temperature limit curves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1)Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response:
        Neither the probability nor the consequences of an accident 
    previously analyzed is increased due to the proposed changes. The 
    adjusted reference temperature of the most limiting beltline 
    material was used to correct the pressure-temperature (P-T) curves 
    to account for irradiation effects. Thus, the operating limits are 
    adjusted to incorporate both the initial fracture toughness 
    conservatism present when the reactor vessel was new and the effect 
    of fluence. The adjusted reference temperature calculations were 
    performed utilizing the guidance contained in RG [Regulatory Guide] 
    1.99, Revision 2. Overpressure Protection System (OPS) curves and 
    tables were regenerated to be consistent with the new P-T curves. 
    The updated curves provide assurance that brittle fracture of the 
    reactor vessel is prevented.
        2) Does the proposed license amendment create the possibility of 
    a new or different kind of accident from any previously evaluated?
        Response:
        The updated P-T and OPS limits will not create the possibility 
    of a new or different kind of accident. The revised operating limits 
    merely update the existing limits by taking into account the effects 
    of radiation embrittlement, utilizing criteria defined in RG 1.99, 
    Revision 2. The updated curves are conservatively adjusted to 
    account for the effect of irradiation on the limiting reactor vessel 
    material.
        No change is being made to the way the pressure-temperature 
    limits provide plant protection. No new modes of operation are 
    involved. Incorporating this amendment does not necessitate physical 
    alteration of the plant.
        3) Does the proposed amendment involve a significant reduction 
    in the margin of safety?
        Response:
        The proposed amendment does not involve a significant reduction 
    in the margin of safety. The pressure-temperature operating limits 
    and OPS setpoints are designed to maintain an appropriate margin of 
    safety. The required margin is specified in ASME [American Society 
    of Mechanical Engineers] Boiler and Pressure Vessel Code, Section 
    III, Appendix G and 10 CFR [Part] 50 Appendix G. The revised curves 
    are based on the latest NRC guidelines along with actual neutron 
    fluence data for the reactor vessel. The new limits retain a margin 
    of safety equivalent to the original margin when the vessel was new 
    and the fracture toughness was slightly greater. The new operating 
    limits account for irradiation embrittlement effects, thereby 
    maintaining a conservative margin of safety.
        The removal of the pressure-temperature limits for criticality 
    does not reduce the plant safety margin because these limits are 
    conservatively encompassed and bounded by the requirements of the 
    proposed Technical Specification 3.1.C.2.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this
    
    [[Page 58902]]
    
    review, it appears that the three standards of 50.92(c) are satisfied. 
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: S. Singh Bajwa, Acting
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: September 6, 1996
        Description of amendment request: The proposed amendments would 
    revise Item 7.c of BVPS-1 Technical Specifications (TSs) Table 3.3-3 
    and Item 7.d of BVPS-2 TS Table 3.3-3 to reflect that a safety 
    injection (SI) signal starts all auxiliary feedwater (AFW) pumps. The 
    notation on BVPS-1 TS Table 3.3-5 would be revised to state that the 
    response time is for all AFW pumps on all SI signal starts. Items 7.d 
    of BVPS-2 TS Tables 3.3-4 and 4.3-2 would be revised to reflect that an 
    SI signal starts all AFW pumps.
        The proposed amendments would also revise and reformat TSs 3/
    4.7.1.2 to more closely resemble the wording contained in the NRC's 
    ``Standard Technical Specifications Westinghouse Plants,'' (NUREG-1431, 
    Revision 1). These changes would require three AFW trains to be 
    operable and would provide what constitutes an operable train. The mode 
    applicability for these TSs would expand to include Mode 4 when the 
    steam generator(s) is relied upon for heat removal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed revisions to reflect that a Safety Injection (SI) 
    signal starts the turbine driven Auxiliary Feedwater (AFW) pump, in 
    addition to both motor driven AFW pumps, will ensure that plant 
    operability requirements for the AFW system actuation signals are 
    maintained at a level consistent with current safety analyses. The 
    proposed revisions to Limiting Condition for Operation (LCO) 3.7.1.2 
    will require that the AFW pumps and associated flow paths are 
    maintained operable to ensure that the AFW system can mitigate the 
    consequences of a Design Basis Accident (DBA) with a loss of normal 
    feedwater. The addition of the Mode 4 applicability will ensure that 
    a safety related source of cooling water is available to remove 
    decay heat.
        The proposed change will ensure that the plant is placed in Mode 
    4 when the number of operable feedwater injection headers is 
    insufficient to ensure that at least two steam generators are 
    supplied during a feedline break accident.
        The proposed addition of footnote (2) to action statement ``c'' 
    will limit plant thermal cycles following a refueling outage due to 
    turbine driven AFW pump inoperability. During the additional time 
    period provided by footnote (2) to reach Hot Shutdown, the two 
    remaining motor driven AFW pumps will provide sufficient flow to the 
    steam generators to mitigate the consequences of a DBA assuming no 
    single failures during this time period. Since there is negligible 
    decay heat following a refueling outage prior to entry into Mode 2, 
    the performance capabilities of the two remaining motor driven AFW 
    pumps to remove decay heat will not be challenged.
        Changing the AFW pump surveillance test frequencies for Beaver 
    Valley Power Station (BVPS) Unit No. 2 to quarterly, as specified in 
    the Inservice Testing (IST) Program, will continue to assure that 
    the AFW system will be capable of performing its intended functions.
        The proposed change to the current Surveillance Requirement 
    4.7.1.2, for BVPS Unit No. 2 only, will not lower the pump 
    performance operability criteria for the AFW pumps. The required 
    values for developed pump head and flow will continue to satisfy 
    accident mitigation requirements and will be maintained and 
    controlled in the BVPS Unit No. 2 IST Program. Future changes to the 
    AFW pump head and flow requirements will be made under the 10 CFR 
    50.59 process to ensure that the AFW design requirement to remove 
    sufficient decay heat continues to be met.
        Based on the above factors, the probability of an accident 
    previously evaluated is not significantly increased.
        The proposed changes do not affect the ability of the AFW system 
    to perform as assumed in the safety analyses. The proposed changes 
    will not result in any additional challenges to plant equipment. 
    Because the plant design limits will continue to be met, the fuel 
    and reactor coolant system pressure boundary integrity is not 
    challenged for the assumptions employed in the calculation of the 
    offsite radiological doses. The additional time to reach Mode 4 from 
    Mode 3 provided by footnote (2) does not result in increased 
    radiological consequences. The potential for a radioactivity release 
    due to the uncontrolled heatup of [the] reactor coolant system[s] 
    are enveloped by the releases postulated in the DBA Loss of Coolant 
    Accident (LOCA) analysis in the Updated Final Safety Analysis 
    Report. The DBA LOCA analysis assumes 102% power operation prior to 
    the event and assumes that core melt occurs. Therefore, there is no 
    increase in the radiological consequences as a result of allowing 
    additional time to repair/test the turbine driven AFW pump. Hence, 
    the consequences of a DBA previously evaluated is not significantly 
    increased.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed change does not alter the method of operating the 
    plant. The AFW system is an accident mitigation system and is 
    normally in standby. System operation is initiated in response to a 
    DBA. The AFW pumps will continue to provide sufficient flow to 
    mitigate the consequences of a DBA. AFW operation continues to 
    fulfill the safety function for which it was designed and no changes 
    to plant equipment will occur. As a result, an accident which is new 
    or different than any already evaluated in the Updated Final Safety 
    Analysis Report will not be created due to this change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes will not affect the heat removal capability 
    of the AFW system to a value less than assumed in the safety 
    analysis. The proposed changes will not result in any additional 
    challenges to the plant equipment including the fuel and reactor 
    coolant system pressure boundary. The additional time period to 
    reach Hot Shutdown provided by footnote (2) will not significantly 
    reduce the decay heat removal capability provided by the AFW system. 
    The two remaining motor driven AFW pumps will continue to provide 
    sufficient flow to the steam generators as assumed in the safety 
    analysis to mitigate the consequences of a DBA assuming no single 
    failure during this time period. The plant will continue to operate 
    within the bounds of the safety analysis.
        The AFW system will continue to be tested in a manner and at a 
    frequency which will ensure acceptable system performance should it 
    be relied upon to remove decay heat following a DBA.
        The AFW pumps' performance requirements will continue to be 
    controlled in a manner to ensure safety analysis assumptions are 
    met.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
    
    [[Page 58903]]
    
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: July 25, 1996
        Description of amendment request: The proposed change modifies 
    Technical Specification (TS) 3/4.7.4 Ultimate Heat Sink (UHS) by 
    incorporating more restrictive fan operability requirements and lower 
    basin temperature. Several other administrative changes are 
    incorporated to improve the humanfactors associated with this TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
    
        Response: No
        The proposed change modifies the UHS TS by revising [Wet Cooling 
    Tower] WCT basin water temperature from less than or equal to 95 
    Degrees Fahrenheit to less than or equal to 89 Degrees Fahrenheit 
    and incorporating more restrictive cooling tower fan operability 
    requirements. These changes are necessary to adequately preserve the 
    assumptions and limits of the revised UHS design basis calculations. 
    These calculations conclude that the UHS is capable of dissipating 
    the maximum peak heat load resulting from the limiting design bases 
    accident (i.e., large break LOCA) and the most severe natural 
    phenomena (i.e., tornado event). Other changes are purely 
    administrative in nature. The proposed change does not directly 
    affect any material condition of the plant that could directly 
    contribute to causing an accident. The proposed change ensures that 
    the mitigating effects of the UHS will be consistent with the design 
    basis analysis. Therefore, the proposed change will not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
    
        Response: No
        The proposed change modifies the UHS TS to be consistent with 
    revised design basis calculations. These new calculations adjust 
    margin to incorporate an additional allowance for fouling in the 
    [Component Cooling Water] CCW heat exchangers and more restrictive 
    UHS minimum fan requirements that were not adequately addressed in 
    the initial design basis. This change also incorporates 
    administrative changes that are intended to improve the application 
    and use of this specification. The proposed change will not alter 
    the operation of the plant or the manner in which the plant is 
    operated. Therefore, the proposed change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
    
        Response: No
        The proposed change modifies the UHS TS by revising WCT basin 
    water temperature from less than or equal to 95 Degrees Fahrenheit 
    to less than or equal to 89 Degrees Fahrenheit and incorporating 
    more restrictive cooling tower fan operability requirements. 
    Modifying the UHS meteorological design bases reduced WCT basin 
    temperature requirement for operability, thus, providing an 
    allowance for fouling in the CCW heat exchangers. The proposed 
    change better preserves the margin of safety by ensuring that the 
    UHS will maintain the CCW accident analysis temperature limit of 115 
    Degrees Fahrenheit. Increased cooling tower fan operability 
    requirements will ensure that the expected cooling efficiency is 
    actually available and not unknowingly degraded due to fouling. 
    Other changes requested herein are purely administrative in nature, 
    do no affect safety margins and intended to improve the use and 
    application of this specification. Therefore, the proposed change 
    will not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of amendment request: October 4, 1996
        Description of amendment request: The proposed amendments would 
    incorporate the requirements necessary to change the basis for 
    prevention of criticality in the fuel storage pool. This change would 
    eliminate credit for Boraflex as a neutron absorbing material in the 
    fuel storage pool criticality analysis and would support the storage of 
    fuel with enrichments up to and including 5.0 weight percent U-235 
    rather than the current value of 4.5 weight percent U-235.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        There is no increase in the radiological consequences of 
    accidents previously evaluated in the Vogtle FSAR [Final Safety 
    Analysis Report] with the use of 5.0 weight percent U-235 fuel. 
    Increasing the enrichment up to and including 5.0 weight percent U-
    235 affects the radiological source terms and subsequently the 
    potential releases both normal and accidental. Evaluations performed 
    (WCAP-12610-P-A, Reference 6) considered the source term, gap 
    fraction, normal operating plant releases and the accident doses for 
    a maximum fuel enrichment of 5.0 weight percent U-235. It was 
    concluded that operating with and storing fuel with 5.0 weight 
    percent U-235 enrichment may result in minor increases in the normal 
    annual releases of long half-life fission products that are not 
    significant. Also, the radiological consequences of accidents are 
    minimally affected due to the very small changes in the core 
    inventory and the fact that the currently assumed gap fractions 
    remain bounding.
        The use of the slightly higher enrichment for VEGP [Vogtle 
    Electric Generating Plant] fuel will not result in burnups in excess 
    of those currently allowed for VEGP. The cycle design methods and 
    limits will remain the same as are currently licensed. Therefore the 
    use of fuel with the higher enrichment is not expected to result in 
    operating conditions outside those currently allowed for VEGP.
        There is no increase in the probability of a fuel assembly drop 
    accident in the fuel storage pool when considering the presence of 
    soluble boron in the pool water for criticality control. The 
    handling of the fuel assemblies in the fuel storage pool has always 
    been performed in borated water.
        Fuel assembly placement will be controlled pursuant to approved 
    fuel handling procedures and will be in accordance with the spent 
    fuel rack storage configuration limitations in the COLR [Core 
    Operating Limit Report]. The consequences of a misplaced assembly 
    have been included in the analysis supporting this revision to the 
    Technical Specifications.
        There is no increase in the consequences of the accidental 
    misloading of a spent fuel assembly into the fuel storage pool racks 
    because criticality analyses demonstrate that
    
    [[Page 58904]]
    
    the pool will remain subcritical following an accidental misloading 
    of an assembly even considering a dilution event. The proposed 
    Technical Specifications and COLR limitations will ensure that an 
    adequate fuel storage pool boron concentration will be maintained.
        There is no increase in the probability of the loss of normal 
    cooling to the fuel storage pool water due to the presence of 
    soluble boron in the pool water for subcriticality control, because 
    a high concentration of soluble boron has been maintained in the 
    fuel storage pool water.
        The loss of normal cooling to the fuel storage pool will cause 
    an increase in the temperature of the fuel storage pool water. This 
    will cause a decrease in water density which would normally result 
    in an addition of negative reactivity. However, since Boraflex is 
    not considered to be present, and the fuel storage pool water has a 
    high concentration of boron, a density decrease causes a positive 
    reactivity addition. The amount of soluble boron required to offset 
    this postulated accident was evaluated for the allowed storage 
    configurations. The amount of soluble boron necessary to mitigate 
    these accidents and ensure that the Keff will be maintained 
    less than or equal to 0.95 has been included in the fuel storage 
    pool boron concentration. Because adequate soluble boron will be 
    maintained in the pool water, the consequences of a loss of normal 
    cooling to the fuel storage pool will not be increased.
        Therefore, based on the conclusions of the above analysis, the 
    proposed changes will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The potential for criticality accidents in the fuel storage pool 
    are not new or different types of accidents. It has been reanalyzed 
    in the Criticality Analysis report (Enclosure 5 [of the proposed 
    amendment request]).
        Because soluble boron has been maintained in the fuel storage 
    pool water, the possibility of a fuel storage pool dilution has 
    previously existed. Therefore, the implementation of Technical 
    Specification controls for the soluble boron will not create the 
    possibility of a new or different kind of accidental pool dilution.
        With credit for soluble boron now a major factor in controlling 
    criticality, an evaluation of fuel storage pool dilution events was 
    completed. A generic methodology was applied... to identify 
    potential events which would dilute the soluble boron contained in 
    PWR [pressurized water reactor] fuel storage pools, and to quantify 
    the frequency of those events. This methodology utilized a 
    probabilistic assessment of a composite plant model to calculate the 
    event frequency of a dilution event. The results of the assessment 
    concluded that the event frequency remained less than the NRC Safety 
    Goal Policy Statement target risk objective of IE-6/reactor year.
        Differences between the composite plant described in WCAP-14181 
    and Vogtle relative to the potential sources of pool dilution were 
    addressed in an individual analysis of the Vogtle pool. This 
    analysis was conducted with methodology which closely paralleled 
    that employed in WCAP-14181. That analysis, found in Enclosure 6 [of 
    the licensee's proposed amendment request], concluded that the 
    frequency of pool dilution to the 0.95 Keff boron concentration 
    (1250 ppm) is on the same order of magnitude as reported in WCAP-
    14181 and less than the NRC Safety Goal Policy Statement criterion 
    of 1.0E-6/reactor year.
        Proposed Technical Specifications 3.7.17 and 3.7.18 which ensure 
    the maintenance of the fuel storage pool boron concentration and 
    storage configuration, do not represent new concepts. The actual 
    boron concentration in the fuel storage pool has been maintained at 
    a higher value than the proposed limits for the Unit 1 and 2 fuel 
    storage pools for refueling purposes. The criticality analysis 
    (Enclosure 5 [of the licensee's proposed amendment request]) 
    determined that a boron concentration of 1,100 ppm (Unit 1) and, 
    1,250 ppm (Unit 2) results in a Keff<0.95 including="" all="" the="" calculational="" uncertainties="" and="" additional="" margin="" to="" compensate="" for="" the="" possibility="" of="" loss="" of="" cooling,="" or="" a="" misplaced="" assembly.="" there="" is="" no="" significant="" change="" in="" plant="" configuration,="" equipment="" design,="" or="" usage="" of="" plant="" equipment.="" the="" safety="" analysis="" for="" dilution="" accidents="" has="" been="" expanded;="" however,="" the="" criticality="" analyses="" assure="" that="" the="" pool="" will="" remain="" subcritical="" with="" no="" credit="" for="" soluble="" boron.="" therefore,="" the="" proposed="" changes="" will="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident.="" 3.="" the="" proposed="" change="" does="" not="" result="" in="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" proposed="" technical="" specifications="" 3.7.17="" and="" 3.7.18="" and="" the="" associated="" spent="" fuel="" boron="" concentration="" and="" storage="" limits="" in="" the="" colr="" will="" provide="" adequate="" safety="" margin="" to="" assure="" that="" the="" stored="" fuel="" assembly="" array="" will="" always="" remain="" subcritical.="" those="" limits="" are="" based="" on="" a="" plant="" specific="" criticality="" analysis="" (enclosure="" 5="" [of="" the="" licensee's="" proposed="" amendment="" request])="" performed="" in="" accordance="" with="" the="" westinghouse="" criticality="" analysis="" methodology...="" while="" the="" cricality="" analysis="" utilized="" credit="" for="" soluble="" boron,="" a="" storage="" configuration="" has="" been="" defined="" using="" maximum="" feasible="">eff calculations to ensure that the spent fuel rack Keff 
    will be less than 1.0 with no soluble boron under normal storage 
    conditions and assuming nominal fuel assembly parameters and fuel 
    rack dimensions. Soluble boron credit is used to offset 
    uncertainties, tolerances and off-normal conditions (such as a 
    misplaced assembly) and to provide subcritical margin such that the 
    fuel storage pool Keff is maintained less than or equal to 
    0.95.
        The loss of a considerable amount of soluble boron in the fuel 
    storage pool which could lead to exceeding a Keff of 0.95 
    during accidents and under adverse conditions has been evaluated and 
    shown to be very improbable.
        The combination of the probabilistic evaluation which shows that 
    the dilution of the fuel storage pool is a low probability 
    occurrence, the maximum feasible Keff calculation which shows 
    that the Keff will remain less than 1.0 when flooded with 
    unborated water and assuming nominal fuel assembly parameters and 
    fuel rack dimensions, and the unavailability of the large volumes of 
    water which are necessary to dilute the fuel storage pool, provide a 
    level of safety comparable to the conservative criticality analysis 
    methodology...
        Therefore, the proposed changes in this license amendment will 
    not result in a significant reduction in the plant's margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308
        NRC Project Director: Herbert N. Berkow
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: September 25, 1996
        Description of amendment request: The proposed amendment would (1) 
    revise the required number of operable gaseous radioactivity monitoring 
    system channels and particulate radioactivity monitoring system 
    channels from one in each of the monitoring systems to one in either of 
    the monitoring systems, (2) allow both the gaseous radioactivity 
    monitoring system and the particulate monitoring system to be 
    inoperable for up to 30 days provided that grab samples are obtained 
    and analyzed at least once per 12 hours, and (3) add an action for the 
    loss of all reactor coolant system leakage detection systems (drywell 
    floor sump level monitoring system, gaseous radioactivity monitoring 
    system and particulate radioactivity monitoring system).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    [[Page 58905]]
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The function of the reactor coolant system leakage detection 
    systems is to detect leakage from the reactor coolant pressure 
    boundary so that appropriate actions can be taken before the 
    integrity of the reactor coolant pressure boundary is impaired. In 
    the plant accident analysis, no credit for mitigation of an accident 
    is taken for the reactor coolant system leakage detection systems. 
    These proposed changes do not alter this function, therefore, these 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated?
        The function of the reactor coolant system leakage detection 
    systems is to detect leakage from the reactor coolant pressure 
    boundary so that appropriate actions can be taken before the 
    integrity of the reactor coolant pressure boundary is impaired. 
    These proposed changes do not alter this function; therefore, these 
    changes do not create the possibility of a new or different kind of 
    accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The change to allow both the gaseous and particulate 
    radioactivity monitoring systems to be inoperable at the same time 
    provided a grab sample is obtained and analyzed at least once per 12 
    hours is predicated on the availability of the primary leak 
    detection system (drywell floor sump level monitor system). Since 
    the gaseous and particulate radioactivity monitoring systems are 
    backups to the drywell floor sump level monitoring system, allowing 
    grab samples every 12 hours provides periodic information that is 
    adequate to detect leakage. The addition of the action to require an 
    orderly shutdown of the unit for the loss of all reactor coolant 
    system leakage detection systems does not affect the margin of 
    safety. Therefore, these proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: October 24, 1996
        Description of amendment request: The proposed amendments would 
    change Technical Specification 3/4.7.1.2, ``Auxiliary Feedwater 
    System.'' The changes would revise the 18-month surveillances performed 
    on the system's pumps and valves because testing of the turbine driven 
    Auxiliary Feedwater pump (TDAFWP) can only be performed in higher modes 
    when there is sufficient secondary steam pressure.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The changes proposed on the testing of components in the AFW 
    [Auxiliary Feedwater] System do not affect the operation of the 
    equipment during conditions when they are required to perform their 
    safety function. No physical changes to the plant result from the 
    proposed changes made to the surveillance requirements. The AFW 
    System is used as a backup system upon loss of main feedwater which 
    is analyzed as a Condition II event in the UFSAR [Updated Final 
    Safety Analysis Report] and as such, does not impact the probability 
    of an accident.
        Testing is being performed with the plant in the condition in 
    which the automatic initiation signals would result, that is, with 
    the plant in Hot Standby. The changes do not impact the availability 
    of the AFW System in providing feedwater to the steam generators. 
    The 24 hour duration to perform testing is sufficiently short that 
    it is considered unlikely that a condition requiring AFW initiation 
    would occur with the TDAFWP unable to feed the generators. For such 
    an occurrence, however, the motor driven AFW pumps would be 
    available to mitigate the consequences of the event. This time is 
    less than the 72 hour allowed outage time for an inoperable TDAFWP 
    in Modes 1-3.
        Therefore, the consequences of an accident previously evaluated 
    are not significantly increased.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not involve any modifications to 
    existing plant equipment, do not alter the function of any plant 
    systems, do not introduce any new operating configurations or new 
    modes of plant operation, nor change the safety analyses. Testing of 
    the TDAFWP in Mode 3, Hot Standby, will not impact auxiliary 
    feedwater capability or impact the ability to maintain Reactor 
    Coolant temperature. The proposed changes will, therefore, not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The changes to the valve surveillance does not decrease the 
    scope of the existing testing, but will clarify the automatic valves 
    to be included.
        The time in which testing is performed, within 24 hours of 
    reaching 680 psig steam generator pressure, ensures that testing is 
    performed in a timely manner after attaining the required steam 
    pressure. This does not impose a significant safety impact since the 
    testing is performed within the plant at the zero load conditions 
    prior to increasing reactor power.
        Elimination of the wording ``during shutdown,'' in reference to 
    the time in which the surveillance is performed, is considered 
    editorial and is proposed for consistency with the change made to 
    the pump surveillance requirement.
        All changes are consistent with the intent of Salem's current TS 
    and with the 18 month surveillances specified in NUREG-1431, 
    Revision 1.
        The proposed change, therefore, does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, NJ 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Power Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendment request: September 30, 1996 (TSCR 192)
        Description of amendment request: The proposed amendments would 
    revise Technical Specification (TS) Section 15.3.3, ``Emergency Core 
    Cooling System, Auxiliary Cooling Systems, Air Recirculation Fan 
    Coolers, and Containment Spray,'' TS 15.3.7, ``Auxiliary Electrical 
    Systems,'' and the TS Bases to reflect proposed changes to the limiting 
    conditions for operation, action statements, allowable outage times, 
    and design specifications for the Point Beach Nuclear Plant (PBNP) TS 
    associated with the containment
    
    [[Page 58906]]
    
    accident fan coolers, service water equipment, and normal and emergency 
    power supplies.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of this facility under the proposed Technical 
    Specifications will not create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The probabilities of accidents previously evaluated are based on 
    the probability of initiating events for these accidents. Initiating 
    events for accidents previously evaluated for Point Beach include: 
    Control rod withdrawal and drop, CVCS [chemical volume and control 
    system] malfunction (Boron Dilution), startup of an inactive reactor 
    coolant loop, reduction in feedwater enthalpy, excessive load 
    increase, losses of reactor coolant flow, loss of external 
    electrical load, loss of normal feedwater, loss of all AC power to 
    the auxiliaries, turbine overspeed, fuel handling accidents, 
    accidental releases of waste liquid or gas, steam generator tube 
    rupture, steam pipe rupture, control rod ejection, and primary 
    coolant system ruptures.
        This license amendment request proposes to change the limiting 
    conditions for operation, action statements, allowable outage times, 
    and design specifications for the Point Beach Nuclear Plant 
    Technical Specifications associated with the containment accident 
    fan coolers, service water equipment, and normal and emergency power 
    supplies.
        These proposed changes do not cause an increase in the 
    probabilities of any accidents previously evaluated because these 
    changes will not cause an increase in the probability of any 
    initiating events for accidents previously evaluated. In particular, 
    these changes affect accident mitigation systems and equipment which 
    do not cause accidents.
        The consequences of the accidents previously evaluated in the 
    PBNP FSAR [final safety analysis report] are determined by the 
    results of analyses that are based on initial conditions of the 
    plant, the type of accident, transient response of the plant, and 
    the operation and failure of equipment and systems. The changes 
    proposed in this license amendment request provide appropriate 
    limiting conditions for operation, action statements, and allowable 
    outage times for service water, containment cooling and normal and 
    emergency power supplies.
        The proposed changes affect components that are required to 
    ensure the proper operation of engineered safety features equipment. 
    The proposed changes do not increase the probability of failure of 
    this equipment or its ability to operate as required for the 
    accidents previously evaluated in the PBNP FSAR. The proposed 
    changes that increase the allowed outage times for engineered safety 
    features equipment continue to provide appropriate limitations for 
    these conditions because sufficient equipment is still required to 
    be operable for accident mitigation and the proposed allowed outage 
    times are consistent with currently accepted time periods for these 
    situations.
        Therefore, this proposed license amendment does not affect the 
    consequences of any accident previously evaluated in the Point Beach 
    Nuclear Plant FSAR, because the factors that are used to determine 
    the consequences of accidents are not being changed.
        2. Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        New or different kinds of accidents can only be created by new 
    or different accident initiators or sequences. New and different 
    types of accidents (different from those that were originally 
    analyzed for Point Beach) have been evaluated and incorporated into 
    the licensing basis for Point Beach Nuclear Plant. Examples of 
    different accidents that have been incorporated into the Point Beach 
    licensing basis include anticipated transients without scram and 
    station blackout.
        The changes proposed by this license amendment request do not 
    create any new or different accident initiators or sequences because 
    these changes to limiting conditions for operation, action 
    statements, allowable outage times, and design specifications for 
    service water, containment cooling and normal and emergency power 
    supplies will not cause failures of equipment or accident sequences 
    different than the accidents previously evaluated. Therefore, these 
    proposed Technical Specification changes do not create the 
    possibility of an accident of a different type than any previously 
    evaluated in the Point Beach FSAR.
        3. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The margins of safety for Point Beach are based on the design 
    and operation of the reactor and containment and the safety systems 
    that provide their protection.
        The changes proposed by this license amendment request provide 
    the appropriate limiting conditions for operation, action 
    statements, allowable outage times, and design specifications for 
    service water, containment cooling and normal and emergency power 
    supplies. This ensure that the safety systems that protect the 
    reactor and containment will operate as required. The design and 
    operation of the reactor and containment are not affected by these 
    proposed changes. Therefore, the margins of safety for Point Beach 
    are not being reduced because the design and operation of the 
    reactor and containment are not being changed and the safety systems 
    and limiting conditions of operation for these safety systems that 
    provide their protection that are being changed will continue to 
    meet the requirements for accident mitigation for Point Beach 
    Nuclear Plant.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    NOTICE OF ISSUANCE OF AMENDMENTS TO FACILITY OPERATING LICENSES
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    [[Page 58907]]
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 & 50-
    324, Brunswick Steam Electric Plant, Units 1 & 2, Brunswick County, 
    North Carolina
    
        Date of amendment request: April 2, 1996 (BSEP 96-0123), as 
    supplemented by an earlier submittal dated November 20, 1995 (BSEP 95-
    0535), and by subsequent submittals dated July 1, 1996 (BSEP 96-0242), 
    July 30, 1996 (BSEP 96-0287), August 7, 1996 (BSEP 96-0300), September 
    13, 1996 (BSEP 96-0340), September 20, 1996 (BSEP 96-0348), October 1, 
    1996 (BSEP 96-0362), October 22, 1996 (BSEP 96-0392), October 22, 1996 
    (BSEP 96-0403), and October 29, 1996 (BSEP 96-0412).
        Brief description of amendment: The proposed amendment would modify 
    Facility Operating Licenses Nos. DPR-71 and DPR-62 and the Technical 
    Specifications (TS) for the Brunswick Steam Electric Plant, Units 1 and 
    2, respectively, to authorize an increase in the maximum power level 
    from 2436 megawatts thermal (MWt) to 2558 MWt.
        Date of issuance: November 1, 1996
        Effective date: November 1, 1996
        Amendment No.: 183 (Unit 1); 214 (Unit 2)
        Facility Operating License Nos. DPR-71 and DPR-62: Amendment 
    revises
        Facility Operating License Nos. DPR-71 and DPR-62 and the Technical 
    Specifications.
        Date of initial notice in Federal Register: May 22, 1996 (61 FR 
    25698) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 1, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: August 5, 1994, as supplemented 
    by letters dated November 17, 1994, December 2, 1994, and August 1, 
    1996.
        Brief description of amendment: The amendment revises surveillance 
    intervals for various systems, components and instruments to 
    accommodate a 24-month refueling cycle. These revisions are being made 
    in accordance with the guidance provided by Generic Letter 91-04, 
    ``Changes in Technical Specification Surveillance Intervals to 
    Accommodate a 24-Month Fuel Cycle.''
        Date of issuance: October 30, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 187
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63117) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 30, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of application for amendment: December 11, 1995, as 
    supplemented by letters dated January 15, September 3, October 2, 
    October 18, and October 25, 1996.
        Brief description of amendment: The amendment revises the 
    Administrative Controls section of the TS by deleting or relocating 
    requirements that are adequately controlled by existing regulatory 
    requirements, adding requirements, and editorially restructuring the TS 
    to be consistent with NUREG-1432, ``Standard Technical Specifications, 
    Combustion Engineering Plants.'' In addition, containment leak rate 
    testing requirements are revised to allow the Type A integrated leak 
    rate test to be scheduled in accordance with Option B of 10 CFR Part 
    50, Appendix J. Review of several changes proposed by the licensee have 
    not yet been completed by the staff. The NRC will issue an evaluation 
    of these changes upon completion of staff review.
        Date of issuance: October 31, 1996
        Effective date: October 31, 1996
        Amendment No.: 174
        Facility Operating License No. DPR-20 Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 20, 1996 (61 
    FR 49493). The October 2, October 18, and October 25, 1996, letters 
    provided clarifying information and updated TS pages that were within 
    the scope of the initial application and did not affect the staff's 
    initial proposed no significant hazards consideration determination. 
    Therefore, renoticing was not warranted.The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    October 31,1996. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, IllinoisDate of 
    application for amendments: April 8, 1996, as supplemented on 
    October 14, 1996.
    
        Brief description of amendments: The amendments revise various 
    sections of the Technical Specifications (TS) to reflect the transition 
    of fuel supplier from General Electric (GE) to Siemens Power 
    Corporation (SPC). The amendments revise the definitions, limiting 
    conditions for operation, required actions, or surveillance 
    requirements related to the following fuel thermal limits: Linear Heat 
    Generation Rate, Critical Power Ratio, Minimum Critical Power Ratio, 
    and Average Planar Linear Heat Generation Rate. The previous GE 
    terminology is replaced with vendor independent terms and new, NRC-
    approved methodologies are incorporated. The amendments also include 
    changes to Section 6.0 of the TS to include SPC references, relocate 
    the requirements for the traversing in-core probe system from the TS to 
    the Core Operating Limits Report, and revise the fuel description in TS 
    Section 5.0.
        Date of issuance: October 29, 1996
        Effective date: Immediately, to be implemented prior to startup of 
    Cycle 9 for Unit 1 and Cycle 8 for Unit 2.
        Amendment Nos.: 116, 101
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 22, 1996 (61 FR 
    25699) The October 14, 1996, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    October 29, 1996.No significant hazards consideration comments 
    received: No
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, IllinoisDate of 
    application for amendments: August 16, 1996, as supplemented on 
    October 4, 1996.
    
        Brief description of amendments: The amendments revise the 
    definition of the F* distance by removing the uncertainty
    
    [[Page 58908]]
    
    term from the specified distance and removing the footnote which 
    specifies the time frame for which it is applicable.
        Date of issuance: November 6, 1996
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 174, 161
        Facility Operating License Nos. DPR-39 and DPR-48: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47968) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 6, 1996No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station Units 1 and 2, Lake County, Illinois
    
        Date of application for amendments: September 3, 1996
        Brief description of amendments: The amendments incorporate revised 
    installation procedures for steam generator tube sleeves designed by 
    ABB Combustion Engineering (ABB/CE).
        Date of issuance: October 29, 1996
        Effective date: October 29, 1996
        Amendment Nos.: 173 and 160
        Facility Operating License Nos. DPR-39 and DPR-48: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47966) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 29, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan Date of application for amendment: September 5, 1996 (NRC-
    96-0075), as supplemented by letters dated October 14, October 23, 
    October 29, and October 31, 1996
    
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 2.1.2 to incorporate cycle-specific safety limit 
    minimum critical power ratios (SLMCPRs) for the core that will be 
    loaded for Cycle 6. In addition, TS 3.4.1.1 is revised to delete the 
    specific SLMCPR number and replace it with a reference to TS 2.1.2.
        Date of issuance: November 5, 1996
        Effective date: November 5, 1996, with full implementation within 
    45 days
        Amendment No.: 109
        Facility Operating License No. NPF-43 Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 25, 1996 (61 
    FR 50342) The letters of October 14, 23, 29, and 31, 1996, provided 
    clarifying information and were not outside the scope of the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated November 5, 1996.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: December 14, 1995, as 
    supplemented by letters dated May 16 and August 29, 1996
        Brief description of amendments: The amendments modify the 
    Technical Specifications for diesel generators to incorporate guidance 
    and recommendations contained in NRC Generic Letter (GL) 93-05, ``Line-
    Item Technical Specifications Improvements to Reduce Surveillance 
    Requirements for Testing During Power Operation,'' GL 94-01, ``Removal 
    of Accelerated Testing and Special Reporting Requirements for Emergency 
    Diesel Generators,'' NUREG-1431, ``Revised Standard Technical 
    Specifications for Westinghouse PWRs,'' and NUREG-1366, ``Improvements 
    to Technical Specifications Surveillance Requirements.''
        Date of issuance: October 30, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 155 and 147
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31175) The August 29, 1996, submittal provided additional information 
    that did not change the scope of the December 14, 1995, application and 
    the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 30, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South 
    CarolinaDate of application for amendments: August 12, 1996, as 
    supplemented by letter dated September 10, 1996
    
        Brief description of amendments: The amendments revise the 
    Technical Specifications associated with the containment leak-rate 
    tests by implementing 10 CFR Part 50, Appendix J, Option B, for Type A 
    leak-rate testing.
        Date of issuance: October 30, 1996
        Effective date: As of the date of issuance to be implemented 30 
    days from the date of issuance.
        Amendment Nos.: 218, 218, 215
        Facility Operating License Nos. DPR-38, DPR-47 and DPR-55: 
    Amendments revise the Technical Specifications.
        Date of initial notice in Federal Register: August 28, 1996 (61 FR 
    44356) The September 10, 1996, letter provided additional information 
    that did not change the scope of the August 12, 1996, application and 
    the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 30, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina
        GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
        Date of application for amendment: April 15, 1996 (TSCR No. 244)
        Brief description of amendment: The amendment revises Specification 
    5.3.1.B to allow the shield plug and the associated lifting hardware to 
    be moved over irradiated fuel assemblies that are in a dry shielded 
    canister within the transfer cask in the cask drop protection system.
        Date of Issuance: November 7, 1996, to be implemented within 30 
    days of issuance
        Effective date: November 7, 1996
        Amendment No.: 187
        Facility Operating License No. DPR-16. Amendment revises the 
    Technical Specifications
    
    [[Page 58909]]
    
        Date of initial notice in Federal Register: May 8, 1996 (61 FR 
    20849) The Commission's related evaluation of this amendment and final 
    determination of no significant hazards consideration addressing 
    comments received on the proposed no significant hazards consideration 
    determination are contained in a Safety Evaluation dated November 7, 
    1996.No significant hazards consideration comments received: Yes.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
    
    GPU Nuclear, Inc., Docket No. 50-320, Three Mile Island Nuclear 
    Station, Unit No. 2, (TMI-2), Dauphin County, Pennsylvania
    
        Date of application for amendment: February 6, 1995
        Brief description of amendment: This amendment revised the 
    Technical Specifications by extending the surveillance interval to 
    demonstrate operability of the containment airlocks from quarterly to 
    annually and to decrease the personnel exposure with implementing the 
    surveillance.
        Date of issuance: October 24, 1996
        Effective date: October 24, 1996
        Amendment No.: 51Possession-Only License No. DPR-73: The amendment 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 5, 1996 (61 FR 
    28616) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 24, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 1, 1995, as supplemented by letters 
    dated June 22, August 28, November 22, and December 19, 1995, and 
    January 4, 8 (two letters), and 23, June 27, July 9, August 8, and 
    September 23, 1996.
        Brief description of amendments: The amendments allowed extension 
    of the standby diesel generator allowed outage time to 14 days, and 
    extension of the essential cooling water loop and the essential chilled 
    water loop allowed outage times to 7 days. The amendments also added to 
    Administrative Controls a description of the Configuration Risk 
    Management Program (CRMP) used to assess changes in core damage 
    probability resulting from applicable plant configurations.
        Date of issuance: October 31, 1996
        Effective date: October 31, 1996, to be implemented within 30 days
        Amendment Nos.: 85 and 72
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 31, 1996 (61 FR 
    40019) The additional information contained in the supplemental letters 
    dated August 8 and September 23, 1996, were clarifying in nature and 
    thus, within the scope of the initial notice and did not affect the 
    staff's proposed no significant hazards consideration determination.The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated October 31, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: February 22, 1996, and 
    supplemented July 22, 1996
        Brief description of amendments: The amendments revise the 
    administrative controls section of the technical specifications to 
    change the operator license requirements for operations management.
        Date of issuance: October 29, 1996
        Effective date: October 29, 1996, with full implementation within 
    45 days
        Amendment Nos.: 212 and 197
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 27, 1996 (61 FR 
    13527) The July 22, 1996, submittal was more restrictive than the 
    original submittal and did not change the staff's original no 
    significant hazards consideration determination.The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated October 29, 1996.No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    ConnecticutDate of application for amendment: August 27, 1996
    
        Brief description of amendment: The Technical Specification (TS) 
    amendment clarifies the limiting condition for operation and 
    surveillance requirements to ensure that the appropriate number of 
    charging pumps and high pressure safety injection pumps are operable 
    for reactivity control and reactor coolant system (RCS) makeup 
    requirements, while also limiting the number of operable pumps to 
    ensure that the low temperature overpressure limits will not be 
    exceeded in the event of a mass addition to the RCS during shutdown 
    conditions. The TS Bases remain unchanged as the result of this 
    amendment.
        Date of issuance: October 25, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 205
        Facility Operating License No. DPR-65: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 20, 1996 (61 
    FR 49498) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 25, 1996No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New YorkDate of 
    application for amendment: March 22, 1996, as supplemented October 
    11, 1996
    
        Brief description of amendment: The amendment proposed changes to 
    the Technical Specifications to establish operability requirements for 
    avoidance and protection from thermal hydraulic instabilities to be 
    consistent with Boiling Water Reactor Owners Group long-term solution 
    Option I-D. Editorial changes are also made to support the revised 
    specifications, improve readability of Bases sections, and enhance the 
    presentation of requirements for single loop operation.
        Date of issuance: October 30, 1996
    
    [[Page 58910]]
    
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 236
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 8, 1996 (61 FR 
    20854) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 30, 1996No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: May 30, 1996, as supplemented by 
    letter dated October 11, 1996
        Brief description of amendment: The amendment proposes to eliminate 
    selected response time testing requirements for certain sensors and 
    specified loop instrumentation.
        Date of issuance: October 28, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 235
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34896) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 28, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey Date of application for amendments: July 12, 
    1996, as supplemented September 12, 1996
    
        Brief description of amendments: The amendments revise Technical 
    Specification Table 3.3-3, ``Engineered Safety Feature Actuation System 
    Instrumentation,'' to clarify the setpoint for the interlock designated 
    P-12.
        Date of issuance: November 4, 1996
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos. 185 and 167
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 23, 1996 (61 FR 
    38229) The supplemental letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination nor the Federal Register notice.The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    November 4, 1996.No significant hazards consideration comments 
    received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
        Dated at Rockville, Maryland, this 13th day of November 1996.
        FOR THE NUCLEAR REGULATORY COMMISSION
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II,Office of Nuclear Reactor 
    Regulation
    [FR Doc. 96-29584 Filed 11-18-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Effective Date:
11/1/1996
Published:
11/19/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-29584
Dates:
November 1, 1996
Pages:
58900-58910 (11 pages)
PDF File:
96-29584.pdf