95-28606. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 60, Number 227 (Monday, November 27, 1995)]
    [Notices]
    [Pages 58394-58416]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-28606]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from October 28, 1995, through November 9, 1995. 
    The last biweekly notice was published on Wednesday, November 8, 1995 
    (60 FR 56361).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By December 27, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any 
    
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    limitations in the order granting leave to intervene, and have the 
    opportunity to participate fully in the conduct of the hearing, 
    including the opportunity to present evidence and cross-examine 
    witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket No. 50-317, Calvert Cliffs 
    Nuclear Power Plant, Unit No. 1, Calvert County, Maryland
    
        Date of amendment request: October 20, 1995.
        Description of amendment request: The proposed one-time amendment 
    would revise the Calvert Cliffs Nuclear Power Plant, Unit No. 1, (CC-1) 
    Technical Specifications (TSs) by extending certain 18-month instrument 
    surveillance intervals by a maximum of 39 days to March 31, 1996. The 
    instruments involved are included in the reactor protective system, 
    engineered safety features actuation system, power-operated relief 
    valves, low-temperature overpressure protection system, remote shutdown 
    instruments, post-accident monitoring, radiation monitoring, and 
    containment sump level instruments.
        The Commission issued Amendment No. 208 to Facility Operating 
    License No. DRP-53 and Amendment No. 186 to Facility Operating License 
    No. DRP-69 for the CC-1/2, respectively. The amendments permanently 
    extended the surveillance intervals for the instruments described above 
    from 18 months to 24 months after a specified number of the instruments 
    had been replaced. The amendments were effective immediately and to be 
    implemented on CC-2 within 30 days, but not implemented on CC-1 until 
    its restart after the spring 1996 refueling outage. All of the 
    instruments identified for replacement on CC-2 have been replaced, but 
    those identified for replacement on CC-1 have not been replaced, thus, 
    the reason for the later implementation date. The proposed one-time 
    amendment is needed prior to Amendment No. 208 being implemented 
    because of a change in the refueling schedule. The licensee has 
    provided technical justification to allow operation for an additional 
    short-time period of up to a maximum of 39 days.
        CC-1 was initially scheduled to begin its refueling outage on 
    February 16, 1996, which would have been within the time frame 
    necessary to perform the required 18-month instrument surveillances 
    currently required for the instruments identified above. The licensee 
    has recently rescheduled the refueling outage for CC-1 to start March 
    15, 1996, several months after the initial amendment request and after 
    consultation with the Pennsylvania-New Jersey-Maryland power pool. The 
    revised schedule will allow the maximum use of the available fuel in 
    the CC-1 reactor core and will also allow the unit to operate for an 
    additional period of about 1 month during a period of potentially high 
    power demand. In addition, the delay will allow more time to plan and 
    prepare for the upcoming refueling outage. Performing the required 
    instrument surveillances at power would present an unwarranted 
    personnel safety risk and, in some cases, the surveillances cannot be 
    done during power operation because they would cause a unit trip. This 
    proposed one-time amendment will be superseded by Amendment No. 208 
    when it is implemented.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed one-time change would extend 18-month instrument 
    surveillance intervals by a maximum of 39 days to March 31, 1996, 
    for specific Reactor Protective System (RPS), Engineered Safety 
    Features Actuation System (ESFAS), Power-Operated Relief Valve, Low 
    Temperature Overpressure Protection (LTOP), Remote Shutdown, Post-
    Accident Monitoring (PAM), Radiation Monitoring, and Containment 
    Sump Level instruments.
        The purpose of the RPS is to effect a rapid reactor shutdown if 
    any one or a combination of conditions deviates from a pre-selected 
    operating range. The system functions to protect the core and the 
    Reactor Coolant System (RCS) pressure boundary. The purpose of the 
    ESFAS is to actuate equipment which protects the public and plant 
    personnel from the accidental release of radioactive fission 
    products if an accident occurs, including a loss-of-coolant 
    accident, main steam line break, or loss of feedwater event. The 
    safety features function to localize, control, mitigate, and 
    terminate such incidents in order to minimize radiation exposure to 
    the general public. The PAM instruments provide the Control Room 
    operators with primary information necessary to take manual actions, 
    as necessary, in response to design basis events, and to verify 
    proper system response to plant conditions and operator actions. The 
    purpose of the Remote Shutdown System is to provide plant parameter 
    indications to operators on a Remote Shutdown Panel to be used while 
    placing and maintaining the plant in a safe shutdown condition in 
    the event the Control Room is uninhabitable. The indications are 
    used to verify proper system response to plant conditions and 
    operator actions. The LTOP System protects against RCS 
    overpressurization at low temperatures 
    
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    by a combination of administrative controls and hardware. Power-
    Operated Relief Valves are set to lift before pressurizer safety 
    valves, and subsequently reseat to minimize the release of reactor 
    coolant from the RCS. The Containment Sump High Level Alarm System 
    provides an alarm in the Control Room to provide one of the 
    available indications of excessive RCS leakage during normal plant 
    operation. The Containment Area High Range Radiation Monitoring 
    System provides an indication of high radiation levels in 
    containment.
        Failure of any of these systems is not an initiator for any 
    previously evaluated accident. Therefore, the proposed change would 
    not involve an increase in the probability of an accident previously 
    evaluated.
        Surveillance and maintenance history has demonstrated good 
    capability for identifying adverse operation by individual 
    instruments. Baltimore Gas and Electric Company has the capability 
    to respond to an inoperable instrument by following the Technical 
    Specification Actions for an inoperable instrument or by performing 
    a channel calibration with the Unit at full power. However, 
    calibration of all the instruments at power is not desirable because 
    of personnel safety, personnel radiation protection goals, and plant 
    reliability concerns.
        These factors provide assurance that the requested surveillance 
    extension will not adversely affect our ability to detect 
    degradation of the instruments. Also, either analysis is available 
    to show the instruments will operate properly during the requested 
    surveillance extension, or the surveillance program has shown that 
    problems will be identified and addressed appropriately. Therefore, 
    these channels will be able to perform the functions assumed in the 
    safety analysis, and there is no significant increase in the 
    consequences of an accident previously evaluated.
        Therefore, the proposed Technical Specification changes do not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        This requested increase in surveillance interval for RPS, ESFAS, 
    Power-Operated Relief Valve, LTOP, Remote Shutdown, PAM, Radiation 
    Monitoring, and Containment Sump Level instrument surveillances does 
    not involve a significant change in the design or operation of the 
    plant. No plant hardware is being modified as part of the proposed 
    change. The proposed change also does not involve any new or unusual 
    actions by plant operators. Therefore, this change would not create 
    the possibility of a new or different type of accident from any 
    accident previously evaluated.
        3. Does operation of the facility in accordance with the 
    proposed amendment involve a significant reduction in a margin of 
    safety?
        The RPS, ESFAS, Power-Operated Relief Valve, LTOP, Remote 
    Shutdown, PAM, Radiation Monitoring, and Containment Sump Level 
    instruments are designed to provide actuation signals and/or 
    indications to ensure appropriate action is taken in response to 
    design basis accidents. Channel checks, channel functional tests and 
    routine comparison of the redundant and independent parameter 
    indications provides a reliable indication of instrument operation. 
    Also, either analysis is available to show the instruments will 
    operate properly during the requested surveillance extension, or 
    instrument surveillance program has shown that problems will be 
    identified and addressed appropriately. During the requested 
    extension, these systems will be available to perform the functions 
    assumed in the Safety Analysis. Surveillance and maintenance history 
    have demonstrated good capability for identifying adverse operation 
    by individual instruments. Baltimore Gas and Electric Company has 
    the capability to respond to such adverse operation, including 
    performing channel calibrations at power. However, such work on all 
    the instruments is not desirable because of personnel safety, 
    personnel radiation protection goals, and plant reliability 
    concerns. Extending the surveillance interval provides additional 
    possibility for instrument components to malfunction by means such 
    as drift or instrument failure, which could allow plant parameters 
    to exceed design bases assumptions. We have determined that the 
    effect of the surveillance interval extension on safety is small, 
    and operation of the instruments in the extended interval would not 
    invalidate any assumption in the plant licensing basis.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Units 1 and 2, Ogle County, Illinois, Docket Nos. STN 
    50-456 and STN 50-457, Braidwood Station, Units 1 and 2, Will County, 
    Illinois
    
        Date of amendment request: October 3, 1995.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications (TSs) for both stations to 
    implement 10 of the line item TS improvements recommended in Generic 
    Letter (GL) 93-05, ``Line-Item Technical Specifications Improvements to 
    Reduce Surveillance Requirements for Testing During Power Operation,'' 
    dated September 27, 1993. The proposed changes also include editorial 
    changes on the affected TS pages.
        The proposed changes from GL 93-05 are the following: (1) TS 
    4.1.3.1.2 (GL 93-05, Item 4.2), extending the interval for checking the 
    operability of each full-length rod not fully inserted in the core from 
    31 days to 92 days; (2) Table 4.3-3 (GL 93-05, Item 5.14), extending 
    the interval for the digital channel operational test for radiation 
    monitoring instrumentation in the table from monthly to quarterly; (3) 
    TS 4.4.3.2 (GL 93-05, Item 6.6), extending the interval between current 
    tests of the required groups of pressurizer heaters from 92 days to 
    each refueling outage; (4) TS 4.4.6.2.2.b (GL 93-05, Item 6.1), 
    extending the time the plant may be in cold shutdown before pressure 
    isolation valve testing is required, prior to entry into Operational 
    Mode 2, from 72 hours to 7 days; (5) TS 4.5.1.1.b (GL 93-05, Item 7.1), 
    revising the requirement to verify the boron concentration in an 
    accumulator within 6 hours of any volume increase to the accumulator 
    (greater than or equal to 70 gallons) so that the verification is not 
    required when the volume increase is from the refueling water storage 
    tank (RWST) and the RWST has not been diluted since verifying that the 
    boron concentration of the RWST is within the concentration limits for 
    the accumulators; (6) TS 4.6.2.1 (GL 93-05, Item 8.1), extending the 
    interval between tests to verify each containment spray nozzle is 
    unobstructed from 5 years to 10 years; (7) TS 4.6.4.1 (GL 93-05, Item 
    5.4), extending the interval for testing each hydrogen monitor for 
    combustible gas control from 31 days to 92 days for the analog channel 
    operational test, and from 92 days to each refueling outage for channel 
    calibration; (8) TS 4.6.4.2 (GL 93-05, Item 8.5), extending the 
    interval between tests to demonstrate operability of the hydrogen 
    recombiner system from 6 months to once each refueling outage; (9) TS 
    4.7.1.2.1.a (GL 93-05, Item 9.1), extending the interval between tests 
    of the auxiliary feedwater pumps from 31 days to 92 days on a staggered 
    test basis; and (10) TS 4.11.2.6 (GL 93-05, Item 13), extending the 
    interval for determining the quantity of radioactivity contained in 
    each gas decay tank, when radioactivity is being added to the tanks, 
    from 24 hours to 7 days, with the 24-hour frequency maintained during 
    the primary coolant degassing operation. The editorial changes are the 
    following: (1) TS 4.4.6.2.1.c, changes the word ``from'' to the word 
    ``to,'' (2) TS 4.5.1.1.c, the 
    
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    change clarifies that the motor control center compartment is for each 
    accumulator isolation valve, (3) TS 4.5.1.2, deletes the footnote 
    because the operating cycle in the footnote is over for each unit, and 
    (4) TS 4.7.1.2.1.a.2 and 4.7.1.2.1.c, renumbers and rephrases (only TS 
    4.7.1.2.1.a.2) other surveillance requirements for the auxiliary 
    feedwater pumps because of the proposed change to TS 4.7.1.2.1.a to 
    implement GL 93-05, Item 9.1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        A. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The changes are consistent with GL 93-05 and NUREG-1366 
    [''Improvements to Technical Specifications Surveillance 
    Requirements,'' December 1992. In GL 93-05, the staff stated that it 
    concluded, in performing the study documented in NUREG-1366, that 
    safety can be improved, equipment degradation decreased, and an 
    unnecessary burden on licensee personnel eliminated by reducing the 
    frequency of certain testing required in the Technical 
    Specifications during power operation]. The changes eliminate 
    testing that is likely to cause transients or excessive wear of 
    equipment. An evaluation of these changes indicates that there will 
    be a benefit to plant safety. The evaluation, documented in NUREG-
    1366, considered (1) unavailability of safety equipment due to 
    testing, (2) initiation of significant transients due to testing, 
    (3) actuation of engineered safety features that unnecessarily cycle 
    safety equipment, (4) importance to safety of that system or 
    component, (5) failure rate of that system or component, and (6) 
    effectiveness of the test in discovering the failure.
        As a result of the decrease in the testing frequencies, the risk 
    of testing causing a transient and equipment degradation will be 
    decreased, and the reliability of the equipment will not be 
    significantly decreased.
        The initial conditions and methodologies used in the accident 
    analyses remain unchanged. The proposed changes do not change or 
    alter the design assumptions for the systems or components used to 
    mitigate the consequences of an accident. Therefore, accident 
    analyses results are not impacted. Appropriate testing will continue 
    to assure that equipment and systems will be capable of performing 
    the intended function.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        B. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes either modify allowable intervals between 
    certain surveillance tests, delete surveillance requirements, or 
    alter an action statement with regard to the required testing. The 
    proposed changes do not affect the design or operation of any 
    system, structure, or component in the plant. The safety functions 
    of the related structures, systems, or components are not changed in 
    any manner, nor is the reliability of any structure, system, or 
    component reduced by the revised surveillance or testing 
    requirements.
        Appropriate testing will continue to assure that the system is 
    capable of performing its intended function. The changes do not 
    affect the manner by which the facility is operated and do not 
    change any facility design feature, structure, system, or component. 
    No new or different type of equipment will be installed. Since there 
    is no change to the facility or operating procedures, and the safety 
    functions and reliability of structures, systems, or components are 
    not affected, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        C. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        All of the proposed technical specification changes are 
    compatible with plant operating experience and are consistent with 
    the guidance provided in GL 93-05 and NUREG-1366. The changes 
    eliminate unnecessary testing that increases the risk of transients 
    and equipment degradation. There is no impact on safety limits or 
    limiting safety system settings.
        The remaining proposed changes are administrative in nature and 
    have no impact on the margin of safety of any technical 
    specification. They do not affect any plant safety parameters or 
    setpoints.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-373, LaSalle County 
    Station, Units 1, LaSalle County, Illinois
    
        Date of amendment request: October 2, 1995
        Description of amendment request: The proposed amendments would 
    revise Section 3.4.2 to change the safety/relief valve (SRV) safety 
    function lift setting tolerances from +1%, -3% to plus or minus 3% and 
    include as-left SRV safety function lift setting tolerances of plus or 
    minus 1%.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The staff has reviewed the licensee's analysis against 
    the standards of 10 CFR 50.92(c). The NRC staff's review is presented 
    below.
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The probability of an accident previously evaluated will not 
    increase as a result of this change, because the only changes are the 
    tolerances for the SRV opening setpoints and the speed of the reactor 
    core isolation cooling system (RCIC) turbine and pump. Changing the 
    maximum allowable opening setpoint for the SRVs does not cause any 
    accident previously evaluated to occur, or degrade valve or system 
    performance in any way so as to cause an accident to occur with an 
    increased frequency. In addition, the increased speed of the RCIC 
    turbine and pump are within the design limits of the system. RCIC 
    operability and failure probabilities are not impacted by this change.
        The consequences of an ASME Overpressurization Event are not 
    significantly increased and do not exceed the previously accepted 
    licensing criteria for this event. General Electric (GE) has calculated 
    the revised peak vessel pressure for LaSalle Station to be 1341 psig, 
    which is well below the 1375 psig criterion of the ASME Code for upset 
    conditions, referenced in Section 5.2.2, Overpressurization Protection, 
    of the Updated Final Safety Analysis Report (UFSAR), and NUREG-0519 
    (Safety Evaluation Report related to the operation of LaSalle County 
    Station, Units 1 and 2, March 1981), and Section 15.2-4, Closure of 
    Main Steam Isolation Valves (BWR) of NUREG-0800 (Standard Review Plan).
        GE has also performed an analysis of the limiting Anticipated 
    Transient Without Scram (ATWS) event, which is the Main Steam Isolation 
    Valve (MSIV) Closure Event. This analysis calculated the peak vessel 
    pressure to be 1457 psig, which is sufficiently below the 1500 psig 
    criterion of the ASME Code for emergency conditions.
        Per NUREG-0519, listed above, Section 5.4.1, and Technical 
    Specification 4.7.3.b, the RCIC pump is required to develop flow 
    greater than or 
    
    [[Page 58399]]
    equal to 600 gpm in the test flow path with a system head corresponding 
    to reactor vessel operating pressure when steam is supplied to the 
    turbine at 1000 +20, -80 psig. Increasing the turbine and pump speed 
    ensures these criteria will still be met and the consequences of an 
    accident will not increase.
        Therefore, there is not a significant increase in the consequences 
    of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The only physical changes are to increase the allowable tolerances 
    for SRV opening setpoints and to increase the RCIC pump and turbine 
    speeds. These changes do not result in any changed component 
    interactions. The SRVs and RCIC will still provide the functions for 
    which they were designed. Since all of the other systems evaluated will 
    continue to function as intended, the proposed changes do not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    the margin of safety.
        While the calculated peak vessel pressures for the ASME 
    Overpressurization Event and the MSIV closure ATWS Event are larger 
    than that previously calculated without the proposed setpoint tolerance 
    increases, the new peak pressures remain sufficiently below the 
    respective licensing acceptance limits associated with these events. In 
    addition, the actual L1C8 reload analysis of the ASME 
    Overpressurization Event will be verified to be within the licensing 
    acceptance limit for that event prior to Unit 1 Cycle 8 startup, as 
    required in the normal reload 10 CFR 50.59 process. These licensing 
    acceptance limits have been previously evaluated as providing a 
    sufficient margin of safety. For other accidents and transients, the 
    increased setpoint tolerances have a negligible effect on the results, 
    so the margin of safety is preserved.
        The staff has reviewed the amendment request and the licensee's no 
    significant hazards consideration determination. Based on the review 
    and the above discussions, the staff proposes to determine that the 
    proposed changes do not involve a significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of amendment request: October 17, 1995.
        Description of amendment request: The proposed amendment would 
    modify the Palisades Facility Operating License to reference 10 CFR 
    Part 40, allow the use of source materials as reactor fuel, delete 
    references to specific amendments and specific revisions in the listed 
    titles of the Physical Security Plan Suitability Training and 
    Qualification Plan and the Safeguards Contingency Plan, delete 
    paragraph 2.F on reporting requirements, and make minor editorial 
    changes. In addition, the Technical Specifications (TS) would be 
    modified as follows: (1) TS 3.1.2 would be modified to change the 
    pressurizer cooldown limit from 100  deg.F to 200  deg.F/hour; (2) the 
    shield cooling system requirements would be relocated to the Palisades 
    Final Safety Analysis Report (FSAR); (3) several minor editorial 
    changes to various sections of the TS are proposed; and (4) revisions 
    to several TS bases pages are proposed.
        Basis for proposed no significant hazards consideration 
    determination As required by 10 CFR 50.91(a), the licensee has provided 
    its analysis of the issue of no significant hazards consideration, 
    which is presented below:
    
    Administrative Changes
    
        Since these changes have no effect on the physical plant or its 
    operation, they cannot involve a significant increase in the 
    probability or consequences of an accident previously evaluated, 
    create the possibility of a new or different kind of accident from 
    any previously evaluated, or involve a significant reduction in a 
    margin of safety.
    
    Technical Changes
    
        The following evaluation supports the finding that operation of 
    the facility in accordance with the two non-administrative changes 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Use of Source Material as reactor fuel: The use of depleted or 
    natural uranium, defined as ``Source Material'' by 10 CFR 40.4, in 
    addition to the currently allowed ``slightly enriched uranium'' 
    would not affect the physical plant or its operation in any way 
    which could increase the probability of any previously evaluated 
    accident. Its use would not introduce any new kind or additional 
    amount of fission product material. Therefore, use of source 
    material as reactor fuel would not affect the consequences of an 
    accident previously evaluated.
        Restoration of the Pressurizer Cooldown Rate Limit: The 
    Palisades Technical Specifications contain a single limit, item 
    3.1.2 b, for both heatup and cooldown rates for the pressurizer. The 
    October 5, 1994 change request proposed changing that limit from 
    200 deg.F/hour to 100 deg.F/hour solely due to its inconsistency 
    with the pressurizer design analysis. Fatigue calculations in the 
    pressurizer design analysis assumed a heatup rate of 100 deg.F/hour 
    and a cooldown rate of 200 deg.F/hour. Until issuance of Amendment 
    163, the Technical specifications contained a single limit for both 
    heatup and cooldown rates of 200 deg.F/hour. Although the installed 
    equipment is not capable of exceeding the 100 deg.F/hour heatup 
    limit, the October 5, 1994 change request proposed a revised limit 
    to assure that the Technical Specification limit was not less 
    restrictive than the design analysis. The higher pressurizer 
    cooldown rate does not affect the results of our analyses which 
    determined the PCS Pressure-Temperature limits or the [Loss of 
    Temperature Overpressurization] LTOP setting requirements of the 
    Technical Specifications.
        When the change was proposed, it was not realized that the more 
    limiting cooldown rate might adversely, and unnecessarily, affect 
    plant operation. This proposed change to the Technical 
    Specifications would separate the limits for heatup rate and 
    cooldown rate, returning the specified cooldown rate to the original 
    value which was consistent with plant design. The current heatup 
    rate limit, which is also consistent with the design, would be 
    retained. The proposed pressurizer cooldown rate will allow 
    depressurizing of the primary coolant system [PCS] and flooding the 
    pressurizer steam space without undue restriction. The more rapid 
    depressurization would be important in the event of a steam 
    generator tube rupture.
        Therefore, operation of the facility in accordance with the 
    proposed change to the Technical Specifications would not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Use of Source Material as reactor fuel: The use of depleted or 
    natural uranium, defined as ``Source Material'' by 10 CFR 40.4, in 
    addition to the currently allowed ``slightly enriched uranium'' 
    would not affect the design (other than the fuel enrichment), 
    configuration, or operation of the plant. Therefore this change 
    cannot create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Restoration of the Pressurizer Cooldown Rate Limit: The proposed 
    change to the Technical Specifications would bring the plant within 
    the assumptions of the design documents for the pressurizer and in 
    line with the Accident analysis for the rapid reduction of the 
    primary coolant system pressure. With the lower rate specified in 
    the present technical specification, the depressurization of the PCS 
    will be delayed to maintain the lower pressurizer cooldown rate.
        Therefore, operation of the facility in accordance with the 
    proposed change to the 
    
    [[Page 58400]]
    Technical Specifications would not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        Use of Source Material as reactor fuel: The use of depleted or 
    natural uranium, defined as ``Source Material'' by 10 CFR 40.4, in 
    addition to the currently allowed ``slightly enriched uranium'' 
    would not affect the Safety Limits, Limiting Conditions for 
    Operation or other operating limits, or the safety analyses which 
    they support. Therefore, the margin of safety is unaffected.
        Restoration of the Pressurizer Cooldown Rate Limit: The proposed 
    change to the Technical Specifications would bring the plant in line 
    with the design analysis. This will not reduce the margin of safety 
    since the higher rate is the basis for the present margin of safety.
        Therefore, the proposed change to the Technical Specifications 
    would not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: Brian E. Holian, Acting.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: September 20, 1995.
        Description of amendment request: The proposed amendment would 
    allow a one-time extension of the 18-month surveillance intervals 
    contained in the Technical Specifications (TS) related to system 
    testing, instrumentation calibration, component inspection, component 
    testing, response time testing and logic system functional tests for 
    various systems, components and instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed TS changes involve a one-time only change in the 
    surveillance testing intervals to facilitate a one-time only change 
    in the Fermi 2 operating cycle. The proposed TS changes do not 
    physically impact the plant nor do they impact any design or 
    functional requirements of the associated systems. That is, the 
    proposed TS changes do not significantly degrade the performance or 
    increase the challenges of any safety systems assumed to function in 
    the accident analysis. The proposed TS changes affect only the 
    frequency of the surveillance requirements and do not impact the TS 
    surveillance requirements themselves. In addition, the proposed TS 
    changes do not introduce any new accident initiators since no 
    accidents previously evaluated have as their initiators anything 
    related to the change in the frequency of surveillance testing. 
    Also, the proposed TS changes do not significantly affect the 
    availability of equipment or systems required to mitigate the 
    consequences of an accident because of other, more frequent testing 
    or the availability of redundant systems or equipment. Furthermore, 
    a historical review of surveillance test results support the above 
    conclusions. Therefore, the proposed TS changes do not significantly 
    increase the probability or consequences of an accident previously 
    evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes involve a one-time only change in the 
    surveillance testing intervals to facilitate the one-time only 
    change in the Fermi 2 operating cycle. The propose TS changes do not 
    introduce any failure mechanisms of a different type than those 
    previously evaluated since there are no physical changes being made 
    to the facility. In addition, the surveillance test requirements 
    themselves will remain unchanged. Therefore, the proposed TS changes 
    do not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        Although the proposed TS changes will result in an increase in 
    the interval between some surveillance tests, the impact, if any, on 
    system availability is small based on other, more frequent testing 
    or redundant systems or equipment, and there is no evidence of any 
    time dependent failures that would impact the availability of the 
    systems. Therefore, the assumptions in the licensing basis are not 
    impacted, and the proposed TS changes do not significantly reduce a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Project Director: Brian E. Holian, Acting.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: August 8, 1995.
        Description of amendment request: The amendments would revise 
    Technical Specification Section 3/4.4.8, Table 4.4-4, Table Notations, 
    to allow the reactor coolant system gross specific activity measurement 
    method to be changed from the current degassed method to a non-
    degassed, or pressurized dilution, method.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1
    
        The requested amendments will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The amendments will have no effect on the probability of 
    the occurrence of any accident. It has been demonstrated that the 
    results obtained by the pressurized dilution technique are 
    statistically similar to results obtained by the degassed technique. 
    Therefore, implemention of the new method will have no effect 
    insofar as the accuracy of the NC [reactor coolant system] system 
    specific activity determination is concerned. Therefore, there will 
    be no effect upon any accident dose consequences.
    
    Criterion 2
    
        The requested amendments will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. No accident causal mechanisms will be affected by 
    installation of the sampling equipment required by the pressurized 
    dilution technique. Operation of the NC system itself will not be 
    affected by the proposed change in sampling technique. All procedure 
    changes required for implementation of the new sampling method will 
    be made according to the provisions of 10 CFR 50.59. No impact on 
    other areas of plant operations will be generated as a result of the 
    new sampling method.
    
    Criterion 3
    
        The requested amendments will not involve a significant 
    reduction in a margin of safety. No impact on any safety limits will 
    result from the change in sample method from the degassed technique 
    to the pressurized dilution technique. Several benefits will result 
    from the change, 
    
    [[Page 58401]]
    including fewer opportunities for valve mispositionings to occur, as 
    well as reduced radiation exposure to Chemistry technicians. The 
    proposed amendment is consistent with a similar amendment approved 
    by the NRC for McGuire Nuclear Station (Amendment Nos. 66 and 47 for 
    McGuire Units 1 and 2, respectively).
        Based upon the preceding analyses, Duke Power Company concludes 
    that the requested amendments do not involve a significant hazards 
    consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242.
        NRC Project Director: Herbert N. Berkow.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: November 7, 1995.
        Description of amendment request: The proposed change would revise 
    Technical Specification 3/4.5.1 SAFETY INJECTION TANKS (SITs) by 
    increasing the specified range associated with SIT water level and 
    nitrogen cover pressure.
        The current limiting conditions for operation (LCO) for the SIT 
    requires that four SITs be operable with a water volume in the range of 
    1679 cubic feet (78%) to 1807 cubic feet (83.8%) and a nitrogen cover 
    pressure between 600 psig to 625 psig. The proposed change requests an 
    expanded range of 925.6 cubic feet (40%) to 1807 cubic feet (83.8%) for 
    SIT level and 600 psig to 670 psig for SIT pressure indicators.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Operation of the facility in accordance with this change does 
    not involve an increase in the probability of any accident. The SITs 
    are used to mitigate the consequences of an accident and are not 
    accident initiators.
        The proposed change would actually decrease the consequence of 
    events such as LOCA [loss of coolant accident] which would result in 
    rapid RCS [reactor coolant system] depressurization.
        By reducing SIT level, the initial nitrogen gas volume is 
    increased which results in an increase in the SIT flow rate into the 
    RCS for a given RCS pressure transient. This decreases the time 
    required to fill the reactor vessel lower plenum after the end of 
    blowdown. During refill, fuel cladding temperature increases rapidly 
    due to insufficient cooling which is provided solely by rod to rod 
    thermal radiation. Decreasing the refill time therefore, results in 
    lower cladding temperature at the start of core reflood which 
    results in lower Peak Cladding Temperature (PCT) during reflood.
        Increasing the nitrogen cover pressure would also result in 
    increased SIT flow rate and would be beneficial as described above.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequence of any accident.
        The proposed change will not create any new system connections 
    or interactions. Thus, no new modes of failure are introduced. The 
    increased range for SIT pressure and level is actually beneficial in 
    maintaining lower PCT following a LOCA.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        The impact of the proposed changes on the Waterford 3 FSAR 
    [Final Safety Analysis Report] analyses have been evaluated. The AOR 
    [Analysis of Record] shows that PCT and maximum cladding oxidation 
    would increase slightly as a result of this change. However, they 
    both remain below the acceptance criteria values of 2200 degrees 
    fahrenhit and 17% for PCT and maximum cladding oxidation, 
    respectively. The system capabilities to mitigate the consequences 
    of accidents will be the same as they were prior to these changes.
        Therefore, the proposed changes do[es] not involve a reduction 
    in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street NW, Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: August 10, 1995
        Description of amendment request: This amendment would incorporate 
    certain improvements into the Three Mile Island, Unit 1 Technical 
    Specifications consistent with the Standard Technical Specifications 
    for Babcock and Wilcox plants. The requested changes would affect the 
    reactor building isolation instrumentation, sampling frequency for the 
    sodium hydroxide tank, and the surveillance requirements for the plant 
    vital bus batteries.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated. The proposed amendment involves changes to the 
    TMI-1 Technical Specifications [TS] which are consistent with the 
    [Babcock & Wilcox] B&W Standard Technical Specifications ([R]STS), 
    NUREG-1430. This change does not involve any change to system or 
    equipment configuration. The proposed amendment revises certain 
    surveillance requirements, or extends certain surveillance 
    intervals. The reliability of systems and components relied upon to 
    prevent or mitigate the consequences of accidents previously 
    evaluated is not degraded by the proposed changes. Therefore, this 
    change does not involve a significant increase in the probability of 
    occurrence or the consequences of an accident previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The change 
    only involves changes to surveillance requirements that are 
    consistent with RSTS or deletion of requirements which are not 
    appropriate for TS. No new failure modes are created and thus the 
    changes are bounded by accidents previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety. These proposed changes involve deletions of requirements or 
    changes in surveillance requirements consistent with the B&W RSTS. 
    No operating limits are affected and no reduction in the margin of 
    safety is involved.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    [[Page 58402]]
    
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London, Connecticut
    
        Date of amendment request: October 24, 1995.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specification (TS) Surveillance Requirement of 
    Section 4.4.5.1, ``Steam Generators'' and the Bases for Section 3/
    4.4.5, ``Steam Generators.'' Typographical errors in Section 
    4.4.5.1.3.c.1 and Table 4.4-6 are also proposed to be corrected. The 
    proposed amendment would defer the next required surveillance to 
    inspect steam generator tubes from October 20, 1996, to the next 
    refueling outage or no later than October 20, 1997, whichever is 
    earlier.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
        Pursuant to 10 CFR 50.92, NNECO [the licensee] has reviewed the 
    proposed one-time change to extend the maximum allowable inspection 
    interval for steam generator tubes from 24 months to 36 months. 
    NNECO concludes that these changes do not involve a significant 
    hazards consideration since the proposed change satisfies the 
    criteria in 10 CFR 50.92(c). That is, the proposed changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        This change involves one-time deferment of the eddy current 
    inspection of the steam generator tubes until the end of the next 
    refueling outage following the thirteenth fuel cycle, but no longer 
    than 12 months beyond the original due date for the inspection. The 
    steam generator tubes have only been exposed to one operating cycle 
    and are made of thermally treated Alloy 690, one of the most 
    corrosion resistant material currently used in recirculating steam 
    generators. Following the first full fuel cycle of operation, the 
    steam generator tube inspection found the tubes to be in excellent 
    condition (i.e., no repairs were required and there was no evidence 
    of an active degradation mechanism). Accordingly, no significant 
    tube degradation is expected by the end of the thirteenth fuel 
    cycle. Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        This one-time change, allowing the steam generator tubes to be 
    examined at the end of the refueling outage following Cycle 13 does 
    not alter the physical design, configuration, or method of operation 
    of the plant. The extension of the inspection interval is not 
    expected to result in significant steam generator tube degradation. 
    Therefore, the proposed change does not create the possibility of a 
    new or different kind of accident from any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        Steam generator tube degradation occurs primarily during 
    operation. The change to extend the maximum allowable inspection 
    interval for steam generator tubes from 24 months to 36 months will 
    not significantly increase the total operating time during Cycle 13 
    (the plant was in an outage for at least 10 months of the 12 month 
    extension). Therefore, there is no significant effect on the extent 
    and severity of tube degradation. The improved corrosion resistance 
    of the steam generators tubes (thermally treated Alloy 690) 
    minimizes the threat of primary- and secondary-side corrosion. No 
    indications of corrosion have been identified in inspections 
    performed so far. Based on our assessment of the inspection data and 
    corrosion potential, all tubes are expected to be within the 
    Regulatory Guide 1.121, ``Bases for Plugging Degraded PWR Steam 
    Generator Tubes,'' limits by the end of Cycle 13. Also, correction 
    of the typographical errors will improve the fidelity of the 
    specification. Therefore, this change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: May 1, June 14 and 29, July 14, 17, 18, 
    and 26, 1995 with supplemental information provided by letter dated 
    October 20, 1995.
        Description of amendment request: Each proposed amendment would 
    change the surveillance requirement frequency from the current once per 
    18-month interval to once per 24-month which is the current length of a 
    Millstone Unit 3 refueling cycle. The changes pertain to the following 
    equipment:
        May 1, 1995, Flow Paths--Operating; Position Indication System; Rod 
    Drop Time; Seismic Monitoring System; Loose Part Detection System; 
    Quench Spray System; Containment Recirculation Spray System; 
    Containment Isolation Valves. This notice supersedes the notice 
    published in the Federal Register on June 6, 1995 (60 FR 29882) 
    relating to containment isolation valves.
        May 1, 1995, Steam Generator Tube Inspections; 10CFR50, Appendix J, 
    Type B and Type C Tests.
        June 14, 1995, AC Sources Operating; DC Sources Operating; 
    Containment Penetration Conductor Overcurrent Protective Devices; 
    Motor-Operated Valves Thermal Overload Protection.
        June 29, 1995, Electric Hydrogen Recombiners; Auxiliary Feedwater 
    System; Reactor Plant Component Cooling Water System; Service Water 
    System; Snubbers.
        July 14, 1995, ECCS Subsystems--Tavg Greater Than or Equal to 350 
    deg.F; pH Trisodium Phosphate Storage Baskets.
        July 17, 1995, Supplementary Leak Collection and Release System; 
    Control Room Emergency Ventilation System; Control Room Envelope 
    Pressurization System; Auxiliary Building Filter System; Fuel Building 
    Exhaust Filter System.
        July 18, 1995, Reactor Coolant System.
        July 26, 1995; Reactor Trip System Instrumentation; ESFAS 
    Instrumentation; Remote Shutdown Instrumentation; Accident Monitoring 
    Instrumentation; RCS Total Flow Rate; Process and Radiation Monitoring 
    Instrumentation.
        In addition, the specifications are changed from a five-column to a 
    one-column format.
        Basis for proposed no significant hazards consideration 
    determination: The Commission has made a proposed determination that 
    the amendment request involves no significant hazards consideration. 
    Under the Commission's regulations in 10 CFR 50.92, this means that 
    operation of the facility in accordance with the proposed amendment 
    would not (1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated; or (2) create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated; or 
    
    [[Page 58403]]
    (3) involve a significant reduction in a margin of safety. As required 
    by 10 CFR 50.91(a), the licensee has provided its analysis of the issue 
    of no significant hazards consideration. The NRC staff has reviewed the 
    licensee's analysis against the standards of 10 CFR 50.92(c). The NRC 
    staff's review is presented below:
        1. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes to surveillance requirements of the Millstone 
    Unit No. 3 Technical Specifications extend the frequency for checking 
    the operability of the affected components/equipment. The proposal 
    would extend the frequency from at least once per 18 months to at least 
    once each refueling interval (i.e., nominal 24-months).
        Changing the frequency of surveillance requirements from at least 
    once per 18 months to at least once each refueling interval does not 
    change the basis for the frequency. The frequency was chosen because of 
    the need to perform this verification under the conditions that apply 
    during a plant outage, and to avoid the potential of an unplanned 
    transient if the surveillances were conducted with the plant at power.
        The proposed changes do not alter the intent or method by which the 
    surveillances are conducted, do not involve any physical changes to the 
    plant, do not alter the way any structure, system, or component 
    functions, and do not modify the manner in which the plant is operated. 
    As such, the proposed changes in the frequency of surveillance 
    requirements will not degrade the ability of the equipment/components 
    to perform its safety function.
        Additional assurance of the operability of the components/equipment 
    is provided by additional surveillance requirements (e.g., monthly or 
    quarterly surveillances).
        Equipment performance over the last four operating cycles was 
    evaluated to determine the impact of extending the frequency of 
    surveillance requirements. This evaluation included a review of 
    surveillance results, preventive maintenance records, and the frequency 
    and type of corrective maintenance. It concluded that there is no 
    indication that the proposed extension could cause deterioration in the 
    condition or performance of any of the subject components.
        In addition to the substantive changes, there are format changes 
    which are merely editorial and because format changes produce no 
    physical change they do not influence the probability or consequences 
    of accidents.
        Since the proposed changes only affect the surveillance frequency 
    for safety systems that are used to mitigate accidents, the changes 
    cannot affect the probability of any previously analyzed accident. 
    While the proposed changes can lengthen the intervals between 
    surveillances, the increases in intervals has been evaluated and it is 
    concluded that there is no significant impact on the reliability or 
    availability of the safety system and consequently, there is no impact 
    on the consequences on any analyzed accident.
        2. The changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed changes to surveillance requirements of the Millstone 
    Unit No. 3 Technical Specifications extend the frequency for verifying 
    the operability of the affected components/equipment. The proposal 
    would extend the frequency from at least once per 18 months to at least 
    once each refueling interval (nominal 24 months).
        Changing the frequency of surveillance requirements from at least 
    once per 18 months to at least once each refueling interval does not 
    change the basis for the frequency. The frequency was chosen because of 
    the need to perform this verification under the conditions that apply 
    during a plant outage, and to avoid the potential of an unplanned 
    transient if the surveillances were conducted with the plant at power.
        In addition to the substantive changes, there are format changes 
    which are merely editorial and because format changes produce no 
    physical change they do not influence the probability of new or 
    different types of accidents.
        The proposed changes do not alter the intent or method by which the 
    surveillances are conducted, do not involve any physical changes to the 
    plant, do not alter the way any structure, system, or component 
    functions, and do not modify the manner in which the plant is operated. 
    As such, the proposed changes cannot create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The changes do not involve a significant reduction in a margin 
    of safety.
        The proposed changes to surveillance requirements of the Millstone 
    Unit No. 3 Technical Specifications extend the frequency for verifying 
    the operability of the components/equipment. The proposal would extend 
    the frequency from at least once per 18-months to at least once each 
    refueling interval (24-months).
        In addition to the substantive changes, there are format changes 
    which are merely editorial and because format changes produce no 
    physical change they do not influence the margin of safety.
        The proposed changes to surveillance frequency are still consistent 
    with the basis for the frequency, and the intent or method of 
    performing the surveillance is unchanged. Further, the current 
    inservice testing requirements and the previous history of reliability 
    of the system provides assurance that the changes will not affect the 
    reliability of the auxiliary feedwater system. Thus, it is concluded 
    that there is no impact on the margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of amendment requests: September 29, 1995.
        Description of amendment requests: The amendments would add a one-
    time footnote to the Technical Specifications regarding the emergency 
    diesel generator diesel fuel oil storage and transfer system to permit 
    the existing storage tanks to be replaced with double walled tanks and 
    piping that comply with new California regulations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Neither the emergency diesel generators (EDGs) nor the diesel 
    fuel oil (DFO) storage and transfer system is an accident initiator. 
    When performing the modifications to the 
    
    [[Page 58404]]
    DFO storage tanks and transfer piping, administrative compensatory 
    measures will be taken to reduce the potential challenge to the EDGs 
    and to verify the operability of the DFO transfer system. A 
    probabilistic risk assessment (PRA) was performed and demonstrates 
    that the change in core damage frequency associated with taking each 
    DFO storage tank and its associated suction transfer piping out of 
    service for 60 days (total of 120 days for both trains) is not 
    significant considering the compensatory measures which will be 
    taken during the tank replacement period.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Neither the EDGs nor the DFO storage and transfer system is an 
    accident initiator. Temporary DFO storage will be onsite during tank 
    replacement. The fire protection guidelines in Appendix 9.5B of the 
    Updated Final Safety Analysis Report will be complied with in order 
    to ensure temporary DFO storage without risk to plant systems.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes considering implementation of the 
    compensatory measures has been shown to not impair safe operation of 
    the plant. Having one DFO storage tank and associated piping out of 
    service does not reduce the margin of safety since temporary storage 
    of DFO will be maintained onsite and administrative compensatory 
    measures will be taken to minimize the potential impact of this 
    condition. Additionally, delivery of DFO to the site is available 
    within 24 hours if needed.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: William H. Bateman.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of amendment requests: October 4, 1995.
        Description of amendment requests: The amendments would relocate 
    the requirements in ten sub-sections of the Technical Specifications to 
    licensee controlled documents in accordance with the guidance in the 
    Commission's Final Policy Statement and the Commission's revisions to 
    10 CFR 50.36 (60 FR 36959, July 19, 1995) on the content of Technical 
    Specifications and the Standard Technical Specifications, Westinghouse 
    Plants, NUREG-1431, Rev. 1, dated April 1995. The ten sub-sections 
    which the licensee proposes to relocate, without changes to the 
    requirements, to the Updated Final Safety Analysis Report or other 
    controlled documents relate to: boration system flow path, position 
    indication system, rod drop time, seismic instrumentation, chlorine 
    detection system, turbine overspeed protection, containment leakage, 
    containment structural integrity, electrical equipment protective 
    devices and containment penetration conductor overcurrent protective 
    devices.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes simplify the Technical Specifications (TS), 
    meet regulatory requirements for relocated TS, and implement the 
    recommendations of the Commission's Final Policy Statement on TS 
    Improvements and revised 10 CFR 50.36. Future changes to these 
    requirements will be controlled by 10 CFR 50.59. The proposed 
    changes are administrative in nature and do not involve any 
    modifications to any plant equipment or affect plant operation.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are administrative in nature, do not 
    involve any physical alterations to any plant equipment, and cause 
    no change in the method by which any safety-related system performs 
    its function. Also, no changes to the operation of the plant or 
    equipment are involved.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes involve relocating TS requirements to a 
    licensee-controlled document. The requirements to be relocated were 
    identified by applying the criteria endorsed in the Commission's 
    Final Policy Statement, which is included in the new revision of 10 
    CFR 50.36, and are consistent with NUREG-1431, Rev. 1 (Reference 2). 
    Thus, the proposed changes do not alter the basic regulatory 
    requirements and do not affect any safety analysis.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: William H. Bateman.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of amendment request: November 2, 1995.
        Description of amendment request: The proposed amendment would 
    revise Section 5.0, Administrative Controls, of the Trojan Nuclear 
    Plant Technical Specifications, Appendix A to License NPF-1, to reflect 
    changes in the organization of the Portland General Electric Company 
    (PGE) as they apply to oversite and management of the Trojan Nuclear 
    Plant.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The requested license amendment does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The changes in management titles and reporting relationships are 
    administrative in nature, do not alter the intent of the Possession 
    Only License, and do not modify 
    
    [[Page 58405]]
    the present plant systems or adminstrative controls necessary to 
    preserve and protect the integrity of the nuclear fuel at the Trojan 
    Nuclear Plant. The Trojan Site Executive and Plant General Manager 
    will be located at the site and will continue to provide senior 
    management attention to each of the functional areas in the Trojan 
    Nuclear Plant organization during decommissioning of the facility.
        The general classification of accidents for the permanently 
    defueled condition are limited. The three classifications are (1) 
    radioactive release from a subsystem or component, (2) fuel handling 
    accident, and (3) loss of spent fuel decay heat removal capability. 
    The probability of occurrences of consequences from these accidents 
    remain unchanged and are bounded by the current accident analysis. 
    Therefore, the requested changes do not involve a significant 
    increase in the probability or occurrence of an accident previously 
    evaluated.
        2. The requested license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The requested amendment is administrative in nature, does not 
    affect the manner in which systems and components are operated or 
    maintained, and does not alter the intent of the Possession Only 
    License. The accident scenarios associated with the permanently 
    defueled condition are limited to (1) radioactive release from a 
    subsystem or component, (2) fuel handling accident and (3) loss of 
    spent fuel decay heat removal capability. There are no new accident 
    scenarios or failure modes created by the requested administrative 
    changes. Therefore the requested change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The requested license amendment does not involve a 
    significant reduction in a margin of safety.
        The requested amendment is administrative in nature, does not 
    affect the manner in which systems and components are operated or 
    maintained, does not alter the intent of the Possession Only 
    License, nor does it adversely impact previously accepted margins of 
    safety. Therefore, the requested amendment does not involve a 
    significant reduction in margin of safety.
    
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
        Attorney for licensees: Leonard A. Girard, Esq., Portland General 
    Electric Company, 121 S.W. Salmon Street, Portland, Oregon 97204.
        NRR Project Director: Seymour H. Weiss.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of amendment request: October 7, 1995 as supplemented by 
    letter dated October 27, 1995.
        Description of amendment request: The proposed change to Hope Creek 
    Technical Specifications (TSs) 4.8.1.1.2, ``A.C. Sources--Operating'', 
    would replace the reference to a voltage and frequency band for the 10 
    second starting time test with a minimum required voltage and frequency 
    that must be attained within 10 seconds.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will not involve a significant increase in the probability or 
    consequences of an accident [* * *] previously evaluated.
        Since no change is being made to the offsite power supplies, or 
    to any system or component that interfaces with the offsite power 
    supplies, there is no change in the probability of a Loss of Offsite 
    Power Accident.
        Since the proposed change still ensures the surveillance 
    requirements meet the licensing basis and since the full spectrum of 
    loading, unloading and standby testing performed at the 18 month 
    frequency continues to demonstrate the capability of the diesel 
    generators to satisfy onsite power requirements during simulated 
    accident conditions while the monthly testing demonstrates 
    availability, there is no change in the consequences of an accident.
        Since the proposed change will eliminate unnecessary adjustments 
    to the governor controls, the probability of malfunction is 
    potentially reduced.
        This change ensures the surveillance requirements reflect the 
    design basis and provide a basis for consistent timing methodology. 
    Since the proposed change is consistent with the intent of the 
    existing specifications, and with the design basis of the system and 
    since no physical changes are being proposed, no action will occur 
    that will increase the probability or consequences of an accident or 
    malfunction of equipment important to safety. The diesel generators 
    will continue to function as stated in the UFSAR [Updated Final 
    Safety Analysis Report].
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of an accident or 
    malfunction of equipment important to safety previously evaluated.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed change does not result in any design or physical 
    configuration changes to the offsite power supplies or to the diesel 
    generators. Operation in accordance with the proposed change will 
    not impair the diesel generators ability to perform as provided in 
    the design basis. By eliminating unnecessary adjustments to the 
    diesel generator governor control, performance during any accident 
    is potentially enhanced. The diesel generators will continue to 
    function as stated in the UFSAR. Therefore, the proposed change will 
    not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        3. Will not involve a significant reduction in a margin of 
    safety.
        Since the proposed change does not involve the addition or 
    modification of plant equipment, is consistent with the intent of 
    the existing Technical Specifications, meets the intent of 
    applicable Regulatory Guides, and is consistent with the design 
    basis of the diesel generators and the UFSAR, no action will occur 
    that will involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
        Attorney for licensee: M.J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street NW., Washington, DC 20005-3502.
        NRC Project Director: John F. Stolz.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: September 29, 1995.
        Description of amendment request: The proposed amendment would 
    modify Technical Specification (TS) 3/4.4.3, Safety Valves and Pilot 
    Operated Relief Valve--Operating, and associated Bases 3/4.4.2 and 3/
    4.4.3, Safety Valves, to increase the lift setting of the pressurizer 
    code safety valves (PSVs) to [equal to or less than] 2575 psig, which 
    corresponds to a lift setting tolerance of +3% of the nominal lift 
    pressure. Increasing the upper bound of the lift setting tolerance of 
    the PSVs from +1% to +3% will allow normal surveillance testing of the 
    PSVs to be within +3% of the nominal lift setpoint of 2500 psig, which 
    is still acceptable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    
    [[Page 58406]]
    consideration, which is presented below:
    
        Toledo Edison has reviewed the proposed changes and determined 
    that a significant hazards consideration does not exist because 
    operation of the Davis-Besse Nuclear Power Station (DBNPS), Unit No. 
    1 in accordance with these changes would:
        1a. Not involve a significant increase in the probability of an 
    accident previously evaluated because increasing the PSV lift 
    tolerance from +1% to +3% only affects the as-found tolerance of the 
    PSVs. The initial setting tolerance will still be limited to +1%. No 
    hardware modification will be done to the valves which could affect 
    any accident initiators.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because increasing the PSV lift 
    tolerance from +1% to +3% does not affect the radiological releases 
    of any accident previously evaluated in the [Updated Safety Analysis 
    Report] USAR. This is not a hardware modification and the reactor 
    coolant pressure boundary integrity is unaffected.
        2. Not create the possibility of a new kind of accident from any 
    previously evaluated because increasing the PSV lift tolerance from 
    +1% to +3% allows the PSVs to protect the reactor coolant pressure 
    boundary from overpressure transients. This change only affects the 
    allowable lift tolerance. The initial lift setting tolerance is 
    still less than +1%. This change does not modify the valve hardware 
    or alter the operation of the valves. The possibility of the valves 
    spuriously opening during power operation will not be changed. The 
    valve setpoint with a -3% lift tolerance is well above the normal 
    operating conditions and the [reactor coolant system] RCS high 
    pressure trip setpoint.
        3. Not involve a significant reduction in a margin of safety 
    because at the +3% lift tolerance the RCS pressure and the reactor 
    thermal power are still within the USAR acceptance criteria for a 
    control rod withdrawal at low power. This change ensures the 
    Technical Specification lift setpoint tolerances are consistent with 
    the requirements given in the [American Society of Mechanical 
    Engineers] ASME Boiler and Pressure Vessel Code.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: Gail H. Marcus.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: June 21, 1994, as amended by letter 
    dated October 23, 1995.
        Description of amendment request: The proposed amendment would 
    relocate the review and audit requirements of the On-site Review 
    Committee (ORC) and Nuclear Safety Review Board (NSRB) contained in TS 
    6.5.1, TS 6.5.2 and TS 6.5.3 to the Operational Quality Assurance 
    Manual (OQAM). In addition, the proposed amendment would delete 
    reference to the Manager, Nuclear Safety and Emergency Preparedness in 
    TS 6.2.3. A revision to the Index was proposed to reflect the 
    relocations. This amendment request was previously published in the 
    Federal Register on August 31, 1994 (59 FR 45036).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The changes are administrative and equivalent descriptions and 
    requirements for these oversight committees are contained in the 
    OQAM.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        These changes do not involve any physical alterations to the 
    plant. There is no new type of accident or malfunction created and 
    the method and manner of plant operation will not change. The 
    changes are administrative and equivalent descriptions and 
    requirements for these oversight committees are contained in the 
    OQAM.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The margin of safety remains unaffected since no design change 
    is made and plant operation remains the same. The changes are 
    administrative and equivalent descriptions and requirements for 
    these oversight committees are contained in the OQAM.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: William H. Bateman.
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: October 17, 1995.
        Description of amendment request: The proposed change would revise 
    the Technical Specifications (TS) for the North Anna Power Station, 
    Unit No. 2 (NA-2). Specifically, the proposed change would reduce from 
    two to one the minimum number of steam generators (SGs) required to be 
    opened for inspection during the first refueling outage following an SG 
    replacement. TS surveillance requirements 4.4.5.0 through 4.4.5.5 for 
    inspection of the SG tubes ensure that the structural integrity of this 
    portion of the Reactor Coolant System will be maintained. Accordingly, 
    the purpose of TS 4.4.5.1 is to require periodic sample inspections of 
    SGs. The initial inspection after SG replacement combined with the 
    subsequent inservice inspections serve to provide reasonable assurance 
    of detection of structural degradation of the tubes. The proposed TS 
    change does not affect or change this basis. However, the requirement 
    that two SGs would be opened and inspected during the first refueling 
    outage after SG replacement is considered unnecessary.
        The NA-2 SGs were replaced during the first quarter of 1995. The 
    purpose of SG replacement was to restore the integrity of the SG tubes 
    to a level equivalent to new SGs. In reality, replacement SG components 
    incorporate a large number of design improvements which reflect the 
    ``state-of-the-art'' technology that currently exists for SG design. 
    These design improvements will improve the long-term maintainability 
    and reliability of the replacement SGs. These enhancements do not 
    adversely affect the mechanical or thermal-hydraulic performance of the 
    SGs. Thus, the replacement SGs are considered superior to the original 
    SGs in terms of design and materials.
        The proposed TS change does not affect or change any limiting 
    conditions for operation (LCO) or any other surveillance requirements 
    in the TS and the Basis for the surveillance requirement remains 
    unchanged. An inspection of the minimum required number of tubes will 
    still be performed 
    
    [[Page 58407]]
    prior to returning the SGs to service. Although the proposed change 
    reduces the number of SGs required to be opened for inspection, the 
    minimum number of tubes required to be examined during the inspection 
    is not being changed. Thus, the minimum inspected tube population size 
    would not be changed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        We have evaluated the proposed change against the criteria 
    described in 10 CFR 50.92 and concluded that the proposed Technical 
    Specifications change does not pose a significant hazards 
    consideration.
        [1] The proposed Technical Specifications change does not affect 
    the assumptions, design parameters, or results of any UFSAR [Updated 
    Final Safety Analysis Report] accident analysis and the proposed 
    amendment does not add or modify any existing equipment. Therefore, 
    the proposed Technical Specifications change would not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        [2] The proposed change to the Technical Specifications does not 
    involve modifications to any of the existing equipment or affect the 
    operation of any existing systems. The absence of any hardware or 
    software changes means that the accident initiators remain 
    unaffected, so no unique accident possibility is created. Therefore, 
    the proposed Technical Specifications change would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        [3] Although the proposed change will reduce the minimum number 
    of steam generators required to be opened for inspection during the 
    first refueling outage following steam generator replacement, the 
    revised Technical Specification surveillance will continue to ensure 
    that a sampling of steam generator tubes will be inspected. The 
    operability of the steam generators will also continue to be 
    verified by periodic inservice inspections. Therefore, since 
    equipment reliability will be maintained, the proposed Technical 
    Specifications change will not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: October 18, 1995.
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specifications 
    (TS) 3.4, ``Steam and Power Conversion System,'' by modifying and 
    clarifying the operability requirements for the main steam safety 
    valves (MSSVs), the auxiliary feedwater (AFW) System, and the 
    condensate storage tank system.
        The proposed amendment would eliminate inconsistencies within TS 
    Section 3.4 and provide the basis for acceptable operation of the 
    Auxiliary Feedwater System below 15% reactor power. The proposed 
    amendment supersedes in its entirety a previously submitted proposed 
    amendment dated May 20, 1994, which was noticed in the Federal Register 
    on September 28, 1994 (59 FR 49442).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Significant Hazards Determination for Proposed Changes to Technical 
    Specification (TS) 3.4.a ``Main Steam Safety Valves''
    
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Currently, TS 3.4.a.1.A.2 requires five MSSVs to be operable 
    prior to heating the reactor > 350  deg.F. The proposed change 
    requires a minimum of two MSSVs per steam generator to be operable 
    prior to heating the reactor coolant system > 350  deg.F, and five 
    MSSVs per steam generator to be operable prior to reactor 
    criticality. If these conditions cannot be met within 48 hours, 
    within 1 hour action shall be initiated to achieve hot standby 
    within 6 hours, achieve hot shutdown within the following 6 hours, 
    and achieve and maintain the reactor coolant system temperature < 350="" deg.f="" within="" an="" additional="" 12="" hours.="" the="" mssvs="" are="" relied="" upon="" to="" function="" in="" each="" of="" the="" following="" usar="" analyzed="" accidents:="" reactor="" coolant="" pump="" locked="" rotor,="" loss="" of="" external="" electrical="" load,="" loss="" of="" normal="" feedwater,="" uncontrolled="" rod="" cluster="" control="" assembly="" withdrawal,="" steam="" generator="" tube="" rupture,="" and="" anticipated="" transients="" without="" scram.="" in="" a="" subcritical="" condition,="" two="" operable="" mssvs="" are="" capable="" of="" relieving="" the="" maximum="" steam="" generated="" during="" these="" anticipated="" design="" basis="" transient="" events.="" because="" this="" proposed="" ts="" requires="" all="" mssvs="" to="" be="" operable="" prior="" to="" reactor="" criticality,="" there="" will="" be="" no="" adverse="" effect="" on="" the="" health="" and="" safety="" of="" the="" public.="" in="" all="" cases,="" the="" relieving="" capacity="" of="" the="" mssvs="" is="" sufficient="" to="" maintain="" steam="" pressures="" within="" safety="" analysis="" acceptable="" criteria,="" and="" reactor="" criticality="" is="" not="" permitted="" unless="" all="" mssvs="" are="" operable.="" therefore,="" there="" is="" no="" adverse="" effect="" on="" the="" health="" and="" safety="" of="" the="" public="" and="" no="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" 2.="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" proposed="" change="" does="" not="" alter="" the="" plant="" configuration,="" operating="" setpoints,="" or="" overall="" plant="" performance.="" therefore,="" it="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident.="" 3.="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" the="" usar="" safety="" analysis="" assumes="" five="" mssvs="" per="" steam="" generator="" are="" operable.="" however,="" as="" shown="" above,="" this="" change="" results="" in="" no="" steam="" generator="" overpressure="" event="" or="" increase="" in="" the="" radiological="" dose.="" therefore,="" this="" change="" will="" not="" involve="" a="" reduction="" in="" the="" margin="" of="" safety.="" significant="" hazards="" determination="" for="" proposed="" changes="" to="" technical="" specification="" (ts)="" 3.4.b="" ``auxiliary="" feedwater="" system''="" the="" proposed="" changes="" were="" reviewed="" in="" accordance="" with="" the="" provisions="" of="" 10="" cfr="" 50.92="" to="" show="" no="" significant="" hazards="" exist.="" the="" proposed="" changes="" will="" not:="" 1.="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" current="" ts="" 3.4.a.1.a.1="" and="" ts="" 3.4.b="" governing="" auxiliary="" feedwater="" flow="" to="" the="" steam="" generators="" are="" being="" combined="" and="" titled,="" ``auxiliary="" feedwater="" system.''="" this="" change="" is="" consistent="" with="" the="" format="" of="" ``westinghouse="" standard="" technical="" specifications,''="" nureg-1431.="" in="" addition="" to="" the="" formatting="" changes,="" a="" number="" of="" technical="" changes="" are="" being="" proposed.="" these="" are:="" the="" correction="" of="" an="" inconsistency="" between="" current="" ts="" 3.4.a.1.a.1="" and="" current="" ts="" 3.4.b.2.a.="" the="" addition="" of="" a="" seven="" (7)="" day="" limiting="" condition="" for="" operation="" (lco)="" action="" statement="" for="" one="" inoperable="" steam="" supply="" to="" the="" turbine="" driven="" auxiliary="" feedwater="" pump.="" a="" specification="" is="" being="" added="" to="" permit="" any="" of="" the="" following="" conditions="" with="" reactor="" power="" less="" than="" 15%,="" without="" declaring="" the="" corresponding="" afw="" train="" inoperable:="" the="" afw="" pump="" control="" switches="" located="" in="" the="" control="" room="" to="" be="" in="" the="" ``pullout''="" position,="" flow="" control="" valves="" afw-2a="" and="" afw-2b="" to="" be="" in="" a="" throttled="" or="" closed="" position,="" and="" train="" cross-connect="" valves="" afw-10a="" and="" afw-10b="" to="" be="" in="" the="" closed="" position.="" an="" inconsistency="" currently="" exists="" between="" current="" ts="" 3.4.a.1.a.1="" and="" current="" ts="" [[page="" 58408]]="" 3.4.b.2.a.="" ts="" 3.4.a.1.a.1="" requires="" the="" system="" piping="" and="" valves="" directly="" associated="" with="" providing="" auxiliary="" feedwater="" flow="" to="" the="" steam="" generators="" to="" be="" operable,="" with="" a="" corresponding="" 48="" hour="" limiting="" condition="" for="" operation="" (lco)="" action="" statement="" if="" this="" requirement="" is="" not="" met.="" ts="" 3.4.b.2.a="" allows="" one="" auxiliary="" feedwater="" pump="" to="" be="" inoperable="" for="" 72="" hours.="" this="" arrangement="" can="" cause="" a="" conflict="" regarding="" which="" ts="" is="" applicable="" depending="" on="" which="" component="" in="" the="" auxiliary="" feedwater="" flowpath="" to="" the="" steam="" generators="" is="" inoperable.="" by="" moving="" all="" ts="" action="" statements="" to="" ts="" 3.4.b,="" the="" inconsistency="" between="" ts="" 3.4.a.1.a.1="" and="" ts="" 3.4.b.2.a="" will="" be="" eliminated.="" the="" requirement="" to="" maintain="" the="" operability="" of="" the="" system="" piping="" and="" valves="" directly="" associated="" with="" providing="" auxiliary="" feedwater="" flow="" to="" the="" steam="" generators="" remains,="" but="" is="" being="" modified="" to="" prevent="" the="" removal="" of="" both="" afw="" supply="" headers="" from="" service.="" proposed="" ts="" 3.4.b.2.c="" is="" being="" added="" to="" allow="" one="" steam="" supply="" to="" the="" turbine="" driven="" auxiliary="" feedwater="" pump="" to="" be="" inoperable="" for="" seven="" days.="" this="" addition="" is="" consistent="" with="" ``westinghouse="" standard="" technical="" specifications,''="" nureg-1431.="" the="" seven="" day="" completion="" time="" is="" reasonable="" based="" on="" the="" redundant="" steam="" supplies="" to="" the="" pump,="" the="" availability="" of="" the="" redundant="" motor-driven="" afw="" pumps,="" and="" the="" low="" probability="" of="" an="" event="" occurring="" that="" requires="" the="" inoperable="" steam="" supply="" to="" the="" turbine="" driven="" afw="" pump.="" for="" these="" reasons,="" this="" change="" will="" have="" no="" adverse="" effect="" on="" the="" health="" and="" safety="" of="" the="" public.="" proposed="" ts="" 3.4.b.6.a="" and="" b="" permit="" the="" afw="" pump="" control="" switches="" located="" in="" the="" control="" room="" to="" be="" placed="" in="" the="" ``pull="" out''="" position="" and="" valves="" afw-2a="" and="" afw-2b="" to="" be="" in="" a="" throttled="" position="" when="" below="" 15%="" reactor="" power="" without="" declaring="" the="" corresponding="" afw="" train="" inoperable.="" this="" change="" is="" proposed="" to="" resolve="" concerns="" regarding="" the="" cycling="" of="" the="" afw="" pumps="" and="" the="" throttling="" of="" valves="" afw-2a="" and="" afw-2b="" during="" plant="" startups="" and="" shutdowns.="" analysis="" shows="" that="" control="" room="" operators="" have="" a="" minimum="" of="" ten="" minutes="" to="" initiate="" auxiliary="" feedwater="" flow="" after="" a="" design="" basis="" accident="" with="" no="" steam="" generator="" dryout="" or="" core="" damage.="" all="" accidents="" which="" rely="" on="" afw="" flow="" for="" mitigation="" were="" reanalyzed="" to="" support="" this="" change.="" these="" analyses="" were="" completed="" assuming="" an="" initial="" power="" of="" 100%.="" however,="" a="" 15%="" reactor="" power="" restriction="" has="" been="" imposed="" on="" placing="" the="" afw="" pump="" control="" switches="" located="" in="" the="" control="" room="" in="" the="" ``pull="" out''="" position="" and="" throttling="" valves="" afw-2a="" and="" afw-2b.="" this="" restriction="" in="" effect="" limits="" use="" of="" ts="" 3.4.b.6="" to="" plant="" startups,="" shutdowns="" and="" other="" low="" power="" operating="" conditions.="" this="" change="" alters="" the="" assumptions="" of="" the="" safety="" analysis="" for="" the="" small-break="" loss="" of="" coolant="" accident,="" the="" steam="" generator="" tube="" rupture="" and="" the="" loss="" of="" normal="" feedwater="" due="" to="" their="" dependence="" on="" the="" afw="" system="" to="" start="" and="" supply="" afw="" for="" heat="" removal.="" to="" support="" this="" change,="" the="" westinghouse="" electric="" corporation="" performed="" an="" analysis="" of="" the="" small-break="" loss-of-coolant="" accident="" using="" the="" notrump="" code="" assuming="" ten="" minutes="" for="" operator="" action="" to="" initiate="" auxiliary="" feedwater.="" this="" analysis="" resulted="" in="" a="" peak="" cladding="" temperature="" (pct)="" of="" 1053="" deg.f="" from="" an="" initial="" power="" level="" of="" 100%.="" in="" addition,="" all="" other="" acceptance="" criteria="" of="" 10="" cfr="" 50.46="" were="" met.="" this="" large="" margin="" to="" the="" 2200="" deg.f="" pct="" limit="" supports="" ten="" minutes="" for="" operator="" action="" to="" initiate="" auxiliary="" feedwater.="" furthermore,="" wpsc="" has="" analyzed="" the="" loss="" of="" normal="" feedwater="" and="" the="" steam="" generator="" tube="" rupture="" accident="" assuming="" delays="" in="" the="" initiation="" of="" auxiliary="" feedwater.="" the="" loss="" of="" normal="" feedwater="" accident="" with="" a="" ten="" minute="" delay="" in="" the="" initiation="" of="" auxiliary="" feedwater="" does="" not="" result="" in="" any="" adverse="" condition="" in="" the="" core.="" it="" does="" not="" result="" in="" water="" relief="" from="" the="" pressurizer="" safety="" valves,="" nor="" does="" it="" result="" in="" uncovering="" the="" tube="" sheets="" of="" the="" steam="" generators.="" also,="" at="" all="" times="" the="" departure="" from="" nucleate="" boiling="" ratio="" (dnbr)="" remained="" greater="" than="" 1.30.="" the="" steam="" generator="" tube="" rupture="" accident="" with="" no="" auxiliary="" feedwater="" flow="" was="" also="" analyzed.="" the="" results="" of="" this="" analysis="" indicate="" that="" neither="" steam="" generator="" empties="" of="" liquid="" and="" at="" least="" 20="" deg.f="" of="" reactor="" coolant="" system="" subcooling="" is="" maintained="" throughout="" the="" transient.="" also,="" there="" is="" no="" increase="" in="" the="" radiological="" dose="" to="" the="" public.="" ten="" minutes="" is="" an="" acceptable="" time="" for="" operator="" action="" because="" four="" independent="" alarms="" in="" the="" control="" room="" would="" initiate="" operator="" action="" to="" place="" the="" afw="" pump="" control="" switches="" to="" the="" ``auto''="" position="" and="" initiate="" afw="" flow="" to="" the="" steam="" generators="" when="" necessary.="" these="" include="" two="" steam="" generator="" lo="" level="" alarms="" (one="" per="" steam="" generator),="" and="" two="" steam="" generator="" lo-lo="" level="" alarms="" (one="" per="" steam="" generator).="" provisions="" also="" exist="" to="" add="" additional="" low="" level="" alarms="" on="" the="" plant="" process="" computer.="" in="" addition="" to="" these="" alarms,="" control="" room="" operators="" have="" twelve="" other="" indications="" of="" insufficient,="" or="" no,="" afw="" flow="" to="" the="" steam="" generators.="" these="" indications="" include="" three="" auxiliary="" feedwater="" pump="" low="" discharge="" pressure="" alarms="" (one="" per="" afw="" pump),="" two="" auxiliary="" feedwater="" flow="" meters="" (one="" per="" steam="" generator),="" two="" afw="" pump="" motor="" amp="" meters="" (one="" per="" motor-driven="" afw="" pump),="" two="" ``esf="" in="" pullout''="" alarms="" (one="" per="" engineered="" safety="" features="" train)="" and="" three="" pump="" running="" lights="" (one="" per="" afw="" pump).="" the="" ten="" minutes="" for="" operator="" action="" was="" discussed="" in="" a="" telephone="" conversation="" between="" wpsc="" and="" mr.="" r.="" laufer="" (nrr).="" ten="" minutes="" for="" operator="" action="" is="" further="" supported="" by="" branch="" technical="" position="" eiscb="" 18.="" scenarios="" have="" been="" completed="" on="" the="" knpp="" simulator="" to="" support="" ten="" minutes="" for="" operator="" initiation="" of="" afw="" flow.="" in="" all="" cases,="" operators="" manually="" initiated="" afw="" flow="" within="" the="" allowed="" ten="" minutes.="" proposed="" ts="" 3.4.b.6.c="" permits="" valves="" afw-10a="" and="" afw-10b="" to="" be="" in="" the="" closed="" position="" when="" below="" 15%="" reactor="" power="" without="" declaring="" the="" turbine-driven="" afw="" train="" inoperable.="" this="" change="" is="" being="" proposed="" to="" allow="" operational="" flexibility="" of="" the="" afw="" system="" during="" startups="" and="" shutdowns.="" as="" described="" below,="" the="" operability="" of="" the="" turbine-driven="" auxiliary="" feedwater="" train="" is="" independent="" of="" the="" position="" of="" the="" valves="" afw-10a="" and="" afw-10b.="" however,="" the="" operability="" of="" this="" train="" is="" dependent="" on="" the="" ability="" of="" these="" valves="" to="" reposition.="" the="" operability="" of="" the="" afw="" system="" following="" a="" main="" steam="" line="" break="" (mslb)="" was="" reviewed="" in="" our="" response="" to="" ie="" bulletin="" 80-04.="" as="" a="" result="" of="" this="" review,="" requirements="" for="" the="" turbine-driven="" afw="" pump="" were="" originally="" added="" to="" the="" technical="" specifications.="" for="" all="" other="" design="" basis="" accidents,="" the="" two="" motor-driven="" afw="" pumps="" supply="" sufficient="" redundancy="" to="" meet="" single="" failure="" criteria.="" in="" a="" secondary="" line="" break,="" it="" is="" assumed="" that="" the="" pump="" discharging="" to="" the="" intact="" steam="" generator="" fails="" and="" that="" the="" flow="" from="" the="" redundant="" motor-driven="" afw="" pump="" is="" discharging="" out="" the="" break.="" therefore,="" to="" meet="" single="" failure="" criteria="" the="" turbine-driven="" afw="" pump="" was="" added="" to="" technical="" specifications.="" the="" cross-connect="" valves="" (afw-10a="" and="" afw-10b)="" are="" normally="" maintained="" in="" the="" open="" position.="" this="" provides="" an="" added="" degree="" of="" redundancy="" above="" what="" is="" required="" for="" all="" accidents="" except="" for="" a="" mslb.="" during="" a="" mslb,="" one="" of="" the="" cross-connect="" valves="" will="" have="" to="" be="" repositioned="" regardless="" if="" the="" valves="" are="" normally="" open="" or="" closed.="" therefore,="" the="" position="" of="" the="" cross-connect="" valves="" does="" not="" affect="" the="" operability="" of="" the="" turbine-driven="" afw="" train.="" however,="" operability="" of="" the="" train="" is="" dependent="" on="" the="" ability="" of="" the="" valves="" to="" reposition.="" for="" these="" reasons,="" this="" change="" will="" have="" no="" adverse="" effect="" on="" the="" health="" and="" safety="" of="" the="" public="" or="" significantly="" increase="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" in="" the="" usar.="" 2.="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" auxiliary="" feedwater="" system="" is="" required="" to="" mitigate="" the="" consequences="" of="" an="" accident.="" the="" auxiliary="" feedwater="" system="" is="" not="" an="" accident="" initiator.="" therefore,="" the="" proposed="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident.="" 3.="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" this="" change="" alters="" the="" assumptions="" of="" the="" safety="" analysis="" for="" the="" small-break="" loss-of-coolant="" accident,="" the="" steam="" generator="" tube="" rupture="" and="" the="" loss="" of="" normal="" feedwater="" due="" to="" their="" dependence="" on="" the="" afw="" system="" to="" start="" and="" supply="" afw="" flow="" for="" heat="" removal.="" to="" support="" this="" change="" the="" westinghouse="" electric="" corporation="" has="" performed="" an="" analysis="" of="" the="" small-break="" loss-of-coolant="" accident="" using="" the="" notrump="" code="" assuming="" ten="" minutes="" for="" operator="" action="" to="" initiate="" auxiliary="" feedwater.="" this="" analysis="" resulted="" in="" a="" peak="" cladding="" temperature="" (pct)="" of="" 1053="" deg.="" f="" from="" an="" initial="" power="" level="" of="" 100%.="" in="" addition,="" all="" other="" acceptance="" criteria="" of="" 10="" cfr="" 50.46="" were="" met.="" this="" large="" margin="" to="" the="" 2200="" deg.="" f="" pct="" limit="" supports="" ten="" minutes="" for="" operator="" action="" to="" initiate="" auxiliary="" feedwater.="" furthermore,="" wpsc="" has="" analyzed="" the="" loss="" of="" normal="" feedwater="" and="" the="" steam="" generator="" tube="" rupture="" accident="" assuming="" delays="" in="" the="" initiation="" of="" auxiliary="" feedwater.="" the="" loss="" of="" normal="" feedwater="" accident="" with="" a="" ten-minute="" delay="" in="" the="" initiation="" of="" auxiliary="" feedwater="" does="" not="" result="" in="" any="" adverse="" condition="" in="" the="" core.="" [[page="" 58409]]="" it="" does="" not="" result="" in="" water="" relief="" from="" the="" pressurizer="" safety="" valves,="" nor="" does="" it="" result="" in="" uncovering="" the="" tube="" sheets="" of="" the="" steam="" generators.="" also,="" at="" all="" times="" the="" departure="" from="" nucleate="" boiling="" ratio="" (dnbr)="" remained="" greater="" than="" 1.30.="" the="" steam="" generator="" tube="" rupture="" accident="" with="" no="" auxiliary="" feedwater="" flow="" was="" also="" analyzed.="" the="" results="" of="" this="" analysis="" indicate="" that="" neither="" steam="" generator="" empties="" of="" liquid="" and="" at="" least="" 20="" deg.="" f="" of="" reactor="" coolant="" system="" subcooling="" is="" maintained="" throughout="" the="" transient.="" also,="" there="" is="" no="" increase="" in="" the="" radiological="" dose="" to="" the="" public.="" for="" these="" reasons,="" these="" changes="" will="" not="" adversely="" affect="" the="" health="" and="" safety="" of="" the="" public="" or="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" as="" discussed="" in="" the="" safety="" evaluation,="" the="" operability="" of="" the="" turbine-driven="" afw="" train="" is="" independent="" of="" the="" position="" of="" valves="" afw-10a="" and="" afw-10b.="" however,="" the="" operability="" of="" the="" train="" is="" dependent="" on="" the="" ability="" of="" these="" valves="" to="" be="" repositioned.="" therefore,="" the="" proposed="" change="" has="" no="" impact="" on="" the="" accident="" analysis="" and="" no="" effect="" on="" the="" margin="" of="" safety.="" significant="" hazards="" determination="" for="" proposed="" administrative="" changes="" to="" section="" ts="" 3.4,="" ``steam="" and="" power="" conversion="" system''="" the="" proposed="" change="" was="" reviewed="" in="" accordance="" with="" the="" provisions="" of="" 10="" cfr="" 50.92="" to="" show="" no="" significant="" hazards="" exist.="" the="" proposed="" change="" will="" not:="" 1.="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated,="" or="" 2.="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated,="" or="" 3.="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" the="" proposed="" changes="" are="" administrative="" in="" nature="" and="" do="" not="" alter="" the="" intent="" or="" interpretation="" of="" the="" ts.="" therefore,="" no="" significant="" hazards="" exist.="" additionally,="" the="" proposed="" change="" is="" similar="" to="" example="" c.2.e(i)="" in="" 51="" fr="" 7751.="" example="" c.2.e.(i)="" states="" that="" changes="" which="" are="" purely="" administrative="" in="" nature;="" i.e.,="" to="" achieve="" consistency="" throughout="" the="" technical="" specifications,="" correct="" an="" error,="" or="" a="" change="" in="" nomenclature,="" are="" not="" likely="" to="" involve="" a="" significant="" hazard.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" university="" of="" wisconsin,="" cofrin="" library,="" 2420="" nicolet="" drive,="" green="" bay,="" wisconsin="" 54311-7001.="" attorney="" for="" licensee:="" bradley="" d.="" jackson,="" esq.,="" foley="" and="" lardner,="" po="" box="" 1497,="" madison,="" wisconsin="" 53701-1497.="" nrc="" project="" director:="" gail="" h.="" marcus.="" wolf="" creek="" nuclear="" operating="" corporation,="" docket="" no.="" 50-482,="" wolf="" creek="" generating="" station,="" coffey="" county,="" kansas="" date="" of="" amendment="" request:="" october="" 18,="" 1995.="" description="" of="" amendment="" request:="" this="" license="" amendment="" would="" replace="" the="" current="" fuel="" oil="" volume="" requirement="" in="" the="" emergency="" diesel="" generator="" (edg)="" day="" tank="" in="" technical="" specifications="" 3.8.1.1.b.1)="" and="" 3.8.1.2.b.1)="" with="" a="" fuel="" oil="" level="" requirement.="" associated="" surveillance="" requirement="" 4.8.1.1.2.a.1)="" would="" also="" be="" changed="" to="" replace="" the="" requirement="" to="" visually="" check="" the="" fuel="" oil="" level="" in="" the="" day="" tank="" with="" a="" requirement="" to="" verify="" that="" the="" fuel="" oil="" transfer="" pump="" starts="" on="" low="" level="" in="" the="" day="" tank="" standpipe.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" 1.="" the="" proposed="" change="" does="" not="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" the="" proposed="" change="" will="" increase="" the="" minimum="" amount="" of="" diesel="" fuel="" oil="" that="" the="" current="" specifications="" require="" to="" be="" maintained="" in="" the="" edg="" day="" tanks="" for="" standby="" operation.="" this="" change="" reflects="" the="" level="" that="" has="" been="" administratively="" maintained="" since="" the="" beginning="" of="" plant="" operation.="" the="" proposed="" change="" will="" not="" affect="" the="" way="" the="" edg="" is="" operated="" and="" does="" not="" affect="" the="" ability="" of="" the="" edgs="" to="" perform="" their="" safety="" function.="" the="" surveillance="" requirement="" change="" is="" being="" made="" to="" more="" thoroughly="" reflect="" the="" method="" used="" to="" assure="" the="" tank="" level="" is="" being="" properly="" maintained.="" the="" proposed="" change="" will="" not="" require="" the="" edg="" to="" be="" operated="" in="" a="" manner="" different="" than="" that="" for="" which="" it="" was="" designed.="" therefore,="" the="" proposed="" change="" will="" not="" significantly="" increase="" the="" consequences="" of="" an="" accident="" or="" malfunction="" of="" equipment="" important="" to="" safety="" previously="" evaluated="" in="" the="" usar.="" 2.="" the="" proposed="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" there="" are="" no="" active="" components="" being="" added="" whose="" failure="" could="" prevent="" the="" edg="" from="" functioning.="" there="" is="" no="" new="" type="" of="" accident="" or="" malfunction="" being="" created="" and="" the="" method="" and="" manner="" of="" plant="" operation="" remains="" unchanged.="" the="" safety="" design="" bases="" in="" the="" usar="" have="" not="" been="" altered.="" thus,="" this="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" previously="" evaluated.="" no="" new="" or="" different="" accident="" scenarios,="" transient="" precursors,="" failure="" mechanisms,="" or="" limiting="" single="" failures="" will="" be="" introduced="" as="" a="" result="" of="" these="" changes.="" the="" method="" of="" operation="" of="" the="" edgs="" is="" not="" being="" altered,="" and="" the="" fuel="" oil="" transfer="" pumps="" will="" continue="" to="" perform="" the="" same="" function="" they="" currently="" perform.="" therefore,="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" other="" than="" those="" already="" evaluated="" will="" not="" be="" created="" by="" this="" change.="" 3.="" the="" proposed="" change="" does="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" there="" are="" no="" changes="" being="" made="" to="" any="" safety="" limits="" or="" safety="" system="" settings="" that="" would="" adversely="" impact="" plant="" safety.="" although="" the="" minimum="" required="" amount="" of="" fuel="" oil="" specified="" in="" the="" technical="" specifications="" is="" being="" revised,="" this="" amount="" of="" fuel="" oil="" has="" been="" administratively="" controlled="" since="" the="" beginning="" of="" commercial="" operation.="" thus,="" the="" operability="" of="" the="" emergency="" diesel="" generators="" has="" never="" been="" affected="" by="" this="" issue.="" neither="" the="" method="" of="" operation="" of="" the="" edgs="" nor="" their="" safety="" function="" are="" being="" altered="" by="" the="" proposed="" change.="" therefore,="" the="" proposed="" change="" would="" not="" result="" in="" a="" reduction="" in="" a="" margin="" of="" safety.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" locations:="" emporia="" state="" university,="" william="" allen="" white="" library,="" 1200="" commercial="" street,="" emporia,="" kansas="" 66801="" and="" washburn="" university="" school="" of="" law="" library,="" topeka,="" kansas="" 66621.="" attorney="" for="" licensee:="" jay="" silberg,="" esq.,="" shaw,="" pittman,="" potts="" and="" trowbridge,="" 2300="" n="" street,="" n.w.,="" washington,="" d.c.="" 20037.="" nrc="" project="" director:="" william="" h.="" bateman.="" wolf="" creek="" nuclear="" operating="" corporation,="" docket="" no.="" 50-482,="" wolf="" creek="" generating="" station,="" coffey="" county,="" kansas="" date="" of="" amendment="" request:="" october="" 24,="" 1995.="" description="" of="" amendment="" request:="" this="" license="" amendment="" request="" proposes="" to="" revise="" surveillance="" requirement="" 4.7.6.e.4="" to="" reflect="" a="" design="" change,="" scheduled="" to="" be="" installed="" during="" the="" next="" refueling="" outage,="" that="" would="" change="" the="" output="" rating="" of="" the="" charcoal="" filter="" adsorber="" unit="" heater="" in="" the="" pressurization="" portion="" of="" the="" control="" room="" emergency="" ventilation="" system="" (crevs)="" from="" 15="" kw="" to="" 5="" kw.="" proposed="" revisions="" to="" surveillance="" requirements="" 4.7.6.c.2="" and="" 4.7.6.d="" are="" included="" which="" would="" change="" the="" acceptance="" criteria="" for="" the="" testing="" of="" carbon="" samples="" from="" the="" crevs="" charcoal="" adsorbers.="" the="" proposal="" would="" adapt="" astm="" d="" 3803-1989="" as="" the="" laboratory="" testing="" standard="" with="" the="" testing="" to="" be="" performed="" at="" 30="" degrees="" centigrade="" and="" 70="" percent="" [[page="" 58410]]="" relative="" humidity="" for="" a="" methyl="" iodide="" penetration="" of="" 2="" percent.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" 1.="" the="" proposed="" change="" does="" not="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" the="" design="" function="" of="" the="" filter="" adsorber="" unit="" heater="" in="" the="" pressurization="" system="" portion="" of="" crevs="" is="" to="" reduce="" the="" relative="" humidity="" of="" the="" air="" entering="" the="" charcoal="" filter="" beds="" to="" 70%="" relative="" humidity.="" although="" the="" original="" design="" specified="" a="" heater="" with="" a="" rating="" of="" 15="" kw,="" review="" of="" the="" design="" basis="" calculation="" for="" this="" system="" indicates="" that="" only="" 2.09="" kw="" is="" actually="" required="" (including="" applicable="" margins="" to="" allow="" for="" voltage="" variations).="" the="" proposed="" change="" to="" the="" crevs="" heaters'="" output="" rating="" from="" 15="" kw="" to="" 5="" kw="" will="" not="" affect="" the="" method="" of="" operation="" of="" the="" system,="" and="" the="" new="" heater="" capacity="" will="" still="" exceed="" filter="" operational="" requirements="" and="" safety="" margin.="" neither="" the="" heater="" change="" nor="" the="" charcoal="" testing="" protocol="" changes="" will="" affect="" system="" operation="" or="" performance,="" nor="" do="" they="" affect="" the="" probability="" of="" any="" event="" initiators.="" these="" changes="" do="" not="" affect="" any="" engineered="" safety="" features="" actuation="" setpoints="" or="" accident="" mitigation="" capabilities.="" therefore,="" the="" proposed="" changes="" will="" not="" significantly="" increase="" the="" consequences="" of="" an="" accident="" or="" malfunction="" of="" equipment="" important="" to="" safety="" previously="" evaluated="" in="" the="" usar.="" 2.="" the="" proposed="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" requested="" change="" to="" the="" crevs="" heaters'="" output="" rating="" and="" the="" changes="" to="" the="" charcoal="" sample="" testing="" protocol="" will="" not="" affect="" the="" method="" of="" operation="" of="" the="" system,="" and="" the="" new="" heater="" capacity="" will="" still="" exceed="" filter="" operational="" requirements="" and="" safety="" margin="" by="" a="" significant="" amount.="" the="" proposed="" changes="" only="" affect="" the="" heater="" size="" in="" the="" system="" and="" the="" testing="" criteria="" for="" the="" charcoal="" samples.="" no="" new="" or="" different="" accident="" scenarios,="" transient="" precursors,="" failure="" mechanisms,="" or="" limiting="" single="" failures="" will="" be="" introduced="" as="" a="" result="" of="" these="" changes.="" therefore,="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" other="" than="" those="" already="" evaluated="" will="" not="" be="" created="" by="" this="" change.="" 3.="" the="" proposed="" change="" does="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" requested="" change="" to="" the="" crevs="" heaters'="" output="" rating="" will="" reduce="" the="" heater="" output="" of="" the="" system,="" but="" the="" new="" heater="" capacity="" will="" still="" exceed="" filter="" operational="" requirements="" and="" safety="" margin="" by="" a="" significant="" amount.="" in="" addition,="" the="" reduction="" in="" heat="" load="" output="" from="" the="" heater="" will="" increase="" the="" design="" margin="" between="" the="" cooling="" capacity="" of="" the="" system="" air="" conditioning="" units="" and="" the="" building="" heat="" load.="" the="" new="" charcoal="" adsorber="" sample="" laboratory="" testing="" protocol="" is="" more="" stringent="" than="" the="" current="" testing="" practice="" and="" more="" accurately="" demonstrates="" the="" required="" performance="" of="" the="" adsorbers="" following="" a="" design="" basis="" loca="" [loss-of-coolant="" accident].="" therefore,="" these="" changes="" will="" not="" reduce="" the="" margin="" of="" safety="" of="" the="" crevs="" filter="" operation.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" locations:="" emporia="" state="" university,="" william="" allen="" white="" library,="" 1200="" commercial="" street,="" emporia,="" kansas="" 66801="" and="" washburn="" university="" school="" of="" law="" library,="" topeka,="" kansas="" 66621.="" attorney="" for="" licensee:="" jay="" silberg,="" esq.,="" shaw,="" pittman,="" potts="" and="" trowbridge,="" 2300="" n="" street,="" n.w.,="" washington,="" d.c.="" 20037.="" nrc="" project="" director:="" william="" h.="" bateman.="" previously="" published="" notices="" of="" consideration="" of="" issuance="" of="" amendments="" to="" facility="" operating="" licenses,="" proposed="" no="" significant="" hazards="" consideration="" determination,="" and="" opportunity="" for="" a="" hearing="" the="" following="" notices="" were="" previously="" published="" as="" separate="" individual="" notices.="" the="" notice="" content="" was="" the="" same="" as="" above.="" they="" were="" published="" as="" individual="" notices="" either="" because="" time="" did="" not="" allow="" the="" commission="" to="" wait="" for="" this="" biweekly="" notice="" or="" because="" the="" action="" involved="" exigent="" circumstances.="" they="" are="" repeated="" here="" because="" the="" biweekly="" notice="" lists="" all="" amendments="" issued="" or="" proposed="" to="" be="" issued="" involving="" no="" significant="" hazards="" consideration.="" for="" details,="" see="" the="" individual="" notice="" in="" the="" federal="" register="" on="" the="" day="" and="" page="" cited.="" this="" notice="" does="" not="" extend="" the="" notice="" period="" of="" the="" original="" notice.="" north="" atlantic="" energy="" service="" corporation,="" docket="" no.="" 50-443,="" seabrook="" station,="" unit="" no.="" 1,="" rockingham="" county,="" new="" hampshire="" date="" of="" amendment="" request:="" september="" 20,="" 1995.="" description="" of="" amendment="" request:="" the="" proposed="" amendment="" would="" modify="" the="" appendix="" a="" technical="" specifications="" for="" the="" engineered="" safety="" features="" actuation="" system="" (esfas)="" instrumentation.="" specifically,="" the="" proposed="" amendment="" would="" revise="" the="" seabrook="" station="" technical="" specifications="" to="" relocate="" functional="" unit="" 6.b,="" ``feedwater="" isolation--="" low="" rcs="">avg Coincident with a Reactor Trip'' from Technical 
    Specification 3.3.2. ``Engineered Safety Features Actuation System 
    Instrumentation'' to the Seabrook Station Technical Requirements Manual 
    which is a licensee controlled document.
        Date of publication of individual notice in Federal Register: 
    October 24, 1995 (60 FR 54524).
        Expiration date of individual notice: November 24, 1995.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved. 
    
    [[Page 58411]]
    
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of application for amendments: October 25, 1994, as 
    supplemented by letter dated September 11, 1995.
        Brief Description of amendments: The proposed amendments change the 
    Technical Specifications to relocate the remaining Environmental 
    Technical Specifications to other licensee-controlled documents and 
    delete the 30-day reporting requirement for inoperable meteorological 
    instrumentation.
        Date of issuance: November 2, 1995.
        Effective date: November 2, 1995.
        Amendment Nos.: 179 and 210.
        Facility Operating License Nos. DPR-71 and DPR-62. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63113). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois, Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: May 13, 1993 as supplemented 
    August 11 and September 20, 1995.
        Brief description of amendments: The amendments revised Section 3/
    4.6.1.7 of the Technical Specifications, Containment Purge Ventilation 
    System, to allow the simultaneous opening of the 8-inch miniflow purge 
    supply and exhaust valves to ensure the containment atmosphere is 
    conducive to human occupants and to maintain their dose as low as 
    reasonably achievable.
        Date of issuance: November 2, 1995.
        Effective date: November 2, 1995.
        Amendment Nos.: 76, 76, 68, and 68.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 15, 1993 (58 
    FR 48379). The August 11 and September 20, 1995, submittals provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois, Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: September 1, 1995, as 
    supplemented on September 1 (two letters), September 2, September 4, 
    September 8, September 15, September 19, September 20, September 22, 
    October 3, October 7, October 11 (two letters), October 13 (three 
    letters), October 23 and October 26, 1995.
        Brief description of amendments: The amendments revise the steam 
    generator (SG) repair criteria in the Byron, Unit 1 and Braidwood, Unit 
    1 Technical Specifications. These revisions add a set of voltage-based 
    SG tube repair criteria different from those previously added by 
    License Amendment No. 66, dated October 24, 1994, to the Byron 1 TSs 
    and by License Amendment No. 54, dated August 18, 1994, to the 
    Braidwood 1 TSs. The present set of voltage repair limits which are 
    being added to the Byron 1 and Braidwood 1 TSs are applicable only for 
    a specific form of SG tube degradation identified as outer diameter 
    stress corrosion cracking (ODSCC) which is confined entirely within the 
    thickness of the tube support plates (TSPs) in the SGs. The voltage-
    based repair criteria for the cold-leg side of the SGs for SG tubes 
    with ODSCC indications and for SG tubes on the hot-leg side which show 
    significant denting, are consistent with those provided in the NRC 
    staff's guidance contained in Generic Letter 95-05, dated August 3, 
    1994.
        The lower voltage repair limit for the SG tubes with ODSCC 
    indications on the hot-leg side of the SGs have been raised from 1.0 to 
    3.0 volts as measured by a bobbin coil. All bobbin indications below 
    3.0 volts will be allowed to remain in service and all bobbin 
    indications above this limit will be either repaired or removed from 
    service by plugging.
        This revision to the voltage repair limits on the hot-leg side 
    reflects a methodology which is significantly different than that 
    contained in GL 95-05. The principal difference between the methodology 
    being applied for the 3.0 volt criteria on the hot-leg side is that the 
    Commonwealth Edison Company (ComEd) is taking credit for the constraint 
    provided by the TSPs to reduce the probability of SG tube burst in the 
    event of a severe accident (i.e., a main steamline break). This 
    constraint is assured by modifying a limited number of SG tubes so that 
    they provide additional stiffness to the TSPs, thereby reducing to a 
    small amount, their deflection under MSLB blowdown loads.
        Additionally, inspection and reporting requirements are being added 
    to the Byron 1 and Braidwood 1 TSs in support of the revised voltage-
    based repair criteria. Further, the maximum permissible value of the 
    iodine-131 concentration in the primary coolant in the Byron 1 TSs is 
    reduced from 1.0 to 0.35 microcuries per gram of coolant. This is the 
    same value for the iodine-131 primary coolant concentration in the 
    Braidwood 1 TSs. Finally, the Bases sections in the Byron 1 and 
    Braidwood 1 TSs are revised to provide a concise description of the 
    methodology proposed by ComEd in support of its proposed revision of 
    the voltage-based SG tube repair criteria.
        Date of issuance: November 9, 1995.
        Effective date: November 9, 1995.
        Amendment Nos.: 77, 77, 69, and 69.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49963).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 9, 1995. The supplemental 
    submittals listed above provide clarifying technical information that 
    does not affect the initial No Significant Hazards Consideration 
    Determination.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481. 
    
    [[Page 58412]]
    
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of application for amendment: July 5, 1995.
        Brief description of amendment: This amendment revises Section 6.0 
    of the Technical Specifications to incorporate several administrative 
    controls and editorial changes to the Training, Plant Review Committee, 
    and Plant Safety and Licensing staff sections.
        Date of issuance: November 3, 1995.
        Effective date: November 3, 1995.
        Amendment No.: 170.
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39435).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 3, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: April 10, 1995.
        Brief description of amendments: The amendments revise the required 
    number of operable hydrogen igniters to allow removal of two hydrogen 
    igniters serving the lower reactor cavity and incore instrument cable 
    tunnel.
        Date of issuance: October 30, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 136 and 130.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49932).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 30, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: September 13, 1995.
        Brief description of amendments: The amendments modify the notation 
    for the overpower delta temperature reactor trip heatup setpoint 
    penalty coefficient as delineated in Note 3 in Technical Specification 
    Table 2.2-1 in order to make the nomenclature consistent with the 
    Standard Technical Specifications and to facilitate a modification to 
    reduce the reactor coolant system hot leg temperature as planned during 
    the Catawba Unit 2 end-of-cycle 7 refueling outage.
        Date of issuance: October 31, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: 137 and 131.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49933).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: September 1, 1995, as 
    supplemented October 17, 1995.
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) 6.9.1.9 to include references to updated or recently 
    approved methodologies used to calculate cycle-specific limits 
    contained in the Core Operating Limits Report. The subject references 
    have been reviewed and approved by the NRC staff.
        Date of issuance: November 2, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: 138 and 132.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49932). The October 17, 1995, letter provided clarifying information 
    that did not change the scope of the September 1, 1995 application and 
    the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: June 13, 1994, as supplemented 
    by letters dated August 15, 1994, March 23, April 18, July 21, and 
    September 22, 1995.
        Brief description of amendments: The amendments revise the 
    Technical Specifications to increase the initial fuel enrichment limit 
    and establish new loading patterns for new and irradiated fuel in the 
    spent fuel pool to accommodate this increase.
        The March 23, 1995, supplement, which provided additional 
    information that modified the June 13, 1994, application's no 
    significant hazards consideration determination, also revises the TS to 
    (1) change the surveillance requirement for boron concentration in the 
    spent fuel pool (SFP), (2) remove the option to use alternate storage 
    configurations in the SFP and replace it with footnotes, (3) add 
    information contained in the Bases to the footnotes, and (4) change the 
    Bases to discuss the option to use specific analyses on alternate fuel.
        Date of issuance: November 6, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 159 and 141.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8746); and May 8, 1995 (60 FR 22590). The April 18, July 21, and 
    September 22, 1995, letters provided additional clarifying information 
    that did not change the scope of the June 13, 1994, application and the 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 6, 1995, and Environmental 
    Assessment dated August 17, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223. 
    
    [[Page 58413]]
    
    
    Florida Power and Light Company, Docket No. 50-335, St. Lucie Plant, 
    Unit No. 1, St. Lucie County, Florida
    
        Date of application for amendment: May 17, 1995.
        Brief description of amendment: The amendment will extend the 
    applicability of the current Reactor Coolant System (RCS) Pressure/
    Temperature Limits and maximum allowed RCS heatup and cooldown rates to 
    23.6 Effective Full Power Years (EFPY) of operation. In addition, 
    administrative changes were proposed for TS 3.1.2.1 (Boration Systems 
    Flow Paths-Shutdown) and TS 3.1.2.3 (Charging Pump-Shutdown) to clarify 
    the conditions for which a High Pressure Safety Injection pump may be 
    used.
        Date of Issuance: October 27, 1995.
        Effective Date: October 27, 1995.
        Amendment No.: 141.
        Facility Operating License No. DPR-67: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32362).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 27, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: February 28, 1994.
        Brief description of amendments: The amendments delete the minimum 
    frequency criteria prescribed for quality assurance audits from 
    Administrative Controls sections 6.5.2.8 and 6.8.4 of the Technical 
    Specifications (TS). Audit periodicity will thereby be controlled by 
    the program described in the Florida Power and Light Company (FPL) 
    Topical Quality Assurance Report.
        Date of Issuance: October 25, 1995.
        Effective Date: October 25, 1995.
        Amendment Nos.: 140 and 80.
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17599).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 25, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant, Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: July 26, 1995.
        Brief description of amendments: These amendments revise selected 
    line items from NRC Generic Letter 93-05, ``Line-Item Technical 
    Specification Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operation.''
        Date of issuance: October 17, 1995.
        Effective date: October 17, 1995.
        Amendment Nos.: 177 and 171.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47617).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 17, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: December 10, 1993.
        Brief description of amendment: The amendment revises the Cooper 
    Nuclear Station Technical Specifications to change the reporting 
    frequency of the Radioactive Materials Release Report from semiannual 
    to annual and to extend the reporting frequency of the Annual Design 
    Change Report from annual to annually or along with the Updated Safety 
    Analysis Report updates required by 10 CFR 50.71(e). This change 
    reflects revised requirements contained in 10 CFR 50.36a and 10 CFR 
    50.59(b).
        Date of issuance: November 3, 1995.
        Effective date: November 3, 1995.
        Amendment No.: 172.
        Facility Operating License No. DPR-46: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7691).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated Novemver 3, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Auburn Public Library, 118 
    15th Street, Auburn, Nebraska 68305.
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: June 28, 1995.
        Brief description of amendment: The amendment revises the Cooper 
    Nuclear Station Technical Specifications to increase the required 
    reactor pressure vessel boron concentration, to modify the surveillance 
    frequency for standby liquid control system pump operability testing 
    from monthly to quarterly, and to make editorial changes.
        Date of issuance: November 8, 1995.
        Effective date: November 8, 1995.
        Amendment No.: 173.
        Facility Operating License No. DPR-46: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39441).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 8, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Auburn Public Library, 118 
    15th Street, Auburn, Nebraska 68305.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: September 5, 1995.
        Description of amendment request: The amendment modifies the 
    Appendix A Technical Specifications (TSs) for the Turbine Cycle Safety 
    Valves. Specifically, the amendment changes Seabrook Station Appendix A 
    Technical Specification Table 3.7-1 to reduce the Maximum Allowable 
    Power Range Neutron Flux--High Setpoints with Inoperable Main Steam 
    Safety Valves (MSSVs) and Table 3.7-2 to reduce the opening setpoints 
    of the MSSVs. Bases Section 3/4.7.1.1 is changed to include the 
    algorithm used for determining the new setpoint values.
        Date of issuance: November 2, 1995.
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 43.
        Facility Operating License No. NPF-86: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 2, 1995 (60 FR 
    51505). 
    
    [[Page 58414]]
    
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, New Hampshire 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: December 21, 1994, as 
    supplemented February 22, 1995.
        Brief description of amendment: The amendment revises the License 
    Condition C.(3), Fire Protection, and certain of the Technical 
    Specifications (TS) related to fire protection requirements. The 
    amendment changes the TS by relocating them to another controlled 
    document, the Technical Requirements Manual referenced in the Final 
    Safety Analysis Report.
        Date of issuance: November 3, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 191.
        Facility Operating License No. DPR-65: Amendment revised the 
    License and Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6303) The February 22, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 3, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: August 31, 1995.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to remove the phrase ``other than Millstone Unit No. 2'' 
    from the Administrative Controls Section 6.3.1, Item (a). This relates 
    to Amendment No. 178 that changed the Technical Specifications to 
    require an individual who serves as the Operations Manager to either 
    hold a Millstone Unit 2 Senior Reactor Operator (SRO) license or have 
    held an SRO license at another pressurized water reactor other than the 
    Millstone Unit No. 2. If the Operations Manager does not hold a 
    Millstone Unit No. 2 SRO license, then an individual serving as the 
    Assistant Operations Manager would be required to possess an SRO 
    license at Millstone Unit 2.
        Date of issuance: November 2, 1995.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 190.
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49941).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: January 27, 1995.
        Brief description of amendments: The amendments change the Limerick 
    Generating Station Units 1 and 2 Technical Specifications (TS) by 
    eliminating the TS active safety function designation of eight (i.e., 
    four per unit) Drywell Chilled Water System valves.
        Date of issuance: October 30, 1995.
        Effective date: October 30, 1995.
        Amendment Nos.: 103 and 67.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20524).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 30, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: November 23, 1994, as 
    supplemented by letter dated August 31, 1995.
        Brief description of amendment: The proposed changes to the 
    Technical Specifications (TSs) revise TS 4.8.2.1, ``Electrical Power 
    Systems--D.C. Sources,'' Surveillance Requirements, and associated 
    Bases Section 3/4.8.2.
        Date of issuance: October 31, 1995.
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment No.: 87.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39449). The August 31, 1995, letter provided additional and clarifying 
    information that did not change the scope of the November 23, 1994, 
    application and the initial proposed no significant consideration 
    determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: November 28, 1994.
        Brief description of amendment: This amendment revises the 
    technical specifications for the Reactor Coolant System recirculation 
    flow upscale trip function to change the trip setpoint and allowable 
    value to reflect 105% of rated core flow, item one of the above 
    application.
        Date of issuance: October 31, 1995.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 86.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications. 
    
    [[Page 58415]]
    
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39450).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: March 30, 1995, as supplemented 
    August 18, 1995.
        Brief description of amendments: The amendments eliminate the 
    defined term CONTROLLED LEAKAGE, remove Controlled Leakage flow from 
    the Reactor Coolant System Operational Leakage Limiting Condition for 
    Operation (LCO) and establish a new Seal Injection Flow LCO.
        Date of issuance: October 30, 1995.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos.: 178 and 159.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24918). The August 18, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 30, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of application for amendments: August 1, 1995, as supplemented 
    by letter dated October 18, 1995.
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) 3/4.3.2, ``Engineered Safety Features Actuation 
    System Instrumentation,'' Table 3.3-3. Table 3.3-3 includes the 
    requirements for the minimum number of toxic gas isolation system 
    (TGIS) trains operable. These amendments are a one-time-only change to 
    extend the allowed TGIS outage times during the replacement of the 
    existing TGIS instrumentation.
        Date of issuance: November 2, 1995.
        Effective date: November 2, 1995, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 2--Amendment No. 126; Unit 3--Amendment No. 
    115.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47625). The October 18, 1995, supplemental letter provided 
    clarifying information and did not change the initial no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: September 30, 1993 (TS-337).
        Brief Description of amendment: The amendments revise the operating 
    license to reflect issuance of a safety evaluation dated November 2, 
    1995 accepting the revised Appendix R Safe Shutdown Program to 
    accommodate simultaneous power operation of Browns Ferry Units 2 and 3.
        Date of issuance: November 2, 1995.
        Effective Date: November 2, 1995.
        Amendment Nos.: 226, 241 and 200.
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    629).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room Location: Athens Public library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: January 4, 1995 (TS 355).
        Brief Description of amendment: The amendments revise applicability 
    and surveillance requirements for the intermediate power range monitor, 
    average power range monitor (APRM), and APRM Inoperative Trip 
    functions.
        Date of issuance: November 2, 1995.
        Effective Date: November 2, 1995.
        Amendment Nos.: 227, 242 and 201.
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29888).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room Location: Athens Public library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: June 2, 1995 (TS 361/371).
        Brief Description of amendment: The amendments revise the 
    operability definition for residual heat removal service water 
    components for use as a standby coolant supply. The amendments also 
    incorporate related changes to the technical specification Bases which 
    were submitted on October 2, 1995.
        Date of issuance: November 2, 1995.
        Effective Date: November 2, 1995.
        Amendment Nos.: 225, 240 and 199.
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42610).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 2, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room Location: Athens Public library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket No. 50-328, Sequoyah Nuclear Plant, 
    Unit 2, Hamilton County, Tennessee
    
        Date of application for amendment: May 19, 1995; revised September 
    11, 1995 (TS 95-13). 
    
    [[Page 58416]]
    
        Brief description of amendment: The amendment modifies License 
    Condition 2.C.(17) by extending the required surveillance interval to 
    May 18, 1996, for Surveillance Requirement 4.3.2.1.3 for certain 
    specified engineered safety features response time tests.
        Date of issuance: October 30, 1995.
        Effective date: October 30, 1995.
        Amendment No.: 204.
        Facility Operating License No. DPR-79: Amendment revises the 
    operating license.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32372); renoticed September 27, 1995 (60 FR 49948).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 30, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
        Dated at Rockville, Maryland, this 15th day of November 1995.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Deputy Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 95-28606 Filed 11-24-95; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Effective Date:
11/2/1995
Published:
11/27/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-28606
Dates:
November 2, 1995.
Pages:
58394-58416 (23 pages)
PDF File:
95-28606.pdf