95-28835. Report to Congress on Abnormal Occurrences April-June, 1995; Dissemination of Information  

  • [Federal Register Volume 60, Number 227 (Monday, November 27, 1995)]
    [Notices]
    [Pages 58387-58390]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-28835]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Report to Congress on Abnormal Occurrences April-June, 1995; 
    Dissemination of Information
    
        Section 208 of the Energy Reorganization Act of 1974, as amended, 
    requires NRC to disseminate information on abnormal occurrences (AOs) 
    (i.e., unscheduled incidents or events that the Commission determines 
    are significant from the standpoint of public health and safety). 
    During the second quarter of CY 1995, the following incidents at NRC 
    licensed facilities were determined to be AOs and are described below, 
    together with the remedial actions taken. Each event is also being 
    included in NUREG-0090, Vol. 18, No. 2, (``Report to Congress on 
    Abnormal Occurrences: April-June 1995''). This report will be available 
    at NRC's Public Document Room, 2120 L Street NW. (Lower Level), 
    Washington, DC, about three weeks after the publication date of this 
    Federal Register Notice.
    
    Nuclear Power Plants
    
    95-2  Reactor Coolant System Blowdown at Wolf Creek Nuclear Generating 
    Station
    
        One of the AO reporting guidelines notes that major deficiencies in 
    design, construction, use of, or management controls for licensed 
    facilities or material can be considered an AO.
        Date and Place--September 17, 1994; Wolf Creek Nuclear Generating 
    Station, a Westinghouse-designed pressurized water reactor nuclear 
    power plant, operated by Wolf Creek Nuclear Operating Corporation and 
    located about 5.63 kilometers (3.5 miles) northeast of Burlington, 
    Kansas.
        Nature and Probable Consequences--An inadvertent blowdown of 
    approximately 34,868 liters (9200 gallons) of reactor coolant through 
    the residual heat removal (RHR) system to the refueling water storage 
    tank (RWST) occurred because of incompatible, concurrent RHR valve 
    manipulations. At the time of the event, the reactor had been shutdown 
    for 28 hours and was on RHR cooling (2413 kPa gauge and 149 C [350 psi 
    gauge and 300 F]). The event was successfully terminated in 1 minute by 
    operator intervention. There was only minimal interruption to heat 
    removal processes, and no core damage or fission product release 
    occurred. However, if the blowdown continued, the licensee estimated 
    that RHR cooling could have failed in about 3.5 minutes, the RWST 
    header could have filled with steam in about 6 minutes, and uncovering 
    of the core could have begun in about 30 minutes.
        All of the emergency core cooling system (ECCS) pumps take their 
    suction from the RWST header line. If the ECCS pumps were started to 
    mitigate the blowdown after the RWST header filled with steam, a 
    common-mode failure of all ECCS pumps could have occurred as a result 
    of steam binding. The ECCS pumps could also have failed as a result of 
    pressure pulses caused by cold RWST 
    
    [[Page 58388]]
    water collapsing the steam in the RWST and RWST header. If they failed, 
    successful mitigation of such an event would depend on the control room 
    operators' cognitive abilities to establish core heat removal via the 
    steam generators.
        If core damage did occur, then a possibility for a significant 
    offsite release existed because the blowdown path in place at the time 
    bypassed the reactor containment.
        Cause or Causes--This event was attributed to the following three 
    causes:
        (1) Unrecognized design vulnerability--An RHR-RWST connecting line 
    was designed to provide operational convenience for refilling the RWST 
    after a refueling outage, but not for safety purposes. The 
    inappropriate use of this line while on RHR cooling could result in a 
    rapid blowdown event and a subsequent common-mode failure of all ECCS 
    pumps.
        (2) Inappropriate use of the RHR-RWST connecting line--The licensee 
    inappropriately used the RHR-RWST connecting line to increase the boron 
    concentration of the RHR train. (Other boration paths existed that 
    would not have resulted in an inadvertent blowdown.)
        (3) Inadequate work control--The licensee was deficient in the 
    control of maintenance and operational evolutions by allowing 
    incompatible activities to occur simultaneously. The control room crew 
    had ample warning of the potential adverse effects of these activities 
    just prior to the event, but failed to limit the concurrent 
    manipulation of selected RHR valves.
        The licensee also had previous warnings of blowdown events from its 
    experience at Wolf Creek and from the following NRC Information 
    Notices: 90-55, ``Recent Operating Experience on Loss of Reactor 
    Coolant Inventory While in a Shutdown Condition''; and 91-42, ``Plant 
    Outage Events Involving Poor Coordination Between Operations and 
    Maintenance Personnel During Valve Testing and Manipulations.'' The 
    licensee's response to these warnings was that its administrative 
    controls adequately addressed the concerns.
    
    Actions Taken to Prevent Recurrence
    
        Licensee--The licensee implemented the following actions: (1) Chain 
    locked the isolation valve in the RHR-RWST connecting line, and made 
    the plant manager and operations manager solely responsible for access 
    to this valve; (2) removed the use of the RHR-RWST connecting line from 
    the RHR boration procedures; and (3) approached the Westinghouse Owners 
    Group to address the issue generically.
        NRC--NRC issued Information Notice No. 95-03, ``Loss of Reactor 
    Coolant Inventory and Potential Loss of Emergency Mitigation Functions 
    While in a Shutdown Condition,'' to inform all reactor licensees of the 
    circumstances and potential consequences associated with the Wolf Creek 
    event.
    
    95-3 Previously Unidentified Path for the Potential Release of 
    Radioactivity at Millstone Nuclear Power Station Unit 2
    
        One of the AO reporting guidelines notes that a loss of plant 
    capability to perform essential safety functions, such that a potential 
    release of radioactivity in excess of 10 CFR Part 100 guidelines could 
    result from a postulated transient or accident (e.g., loss of emergency 
    core cooling system, loss of control rod system), can be considered an 
    AO.
        Date and Place--December 6, 1994; Millstone Nuclear Power Station 
    Unit 2, a Combustion Engineering-designed pressurized water reactor 
    nuclear power plant, operated by Northeast Nuclear Energy Company and 
    located about 5.15 kilometers (3.2 miles) west-southwest of New London 
    County, Connecticut.
        Nature and Probable Consequences--While the plant was in a 
    refueling outage, a systems engineer employed by the licensee 
    identified a condition that established a potential unfiltered release 
    path to the atmosphere that could have resulted in offsite doses in 
    excess of 10 CFR Part 100 guidelines in the event of a postulated loss-
    of-coolant accident (LOCA). The licensee immediately declared the 
    enclosure building inoperable and promptly reported the condition to 
    NRC.
        The Millstone Unit 2 design includes an Enclosure Building around 
    the reactor Containment Building to collect all leakage out of the 
    containment during a postulated LOCA. The Enclosure Building 
    Ventilation System contains a charcoal bed filtration unit to remove 
    radioactive iodine prior to discharging the Enclosure Building air out 
    of the 114.4-meter (375-foot) high Unit-1 stack. The condition 
    identified on December 6, 1994, was that the ventilation system 
    associated with the Hydrogen Analyzer cabinet and waste gas sample hood 
    fan, located within the East Electrical Penetration Room of the 
    Enclosure Building, would not isolate in the event of a LOCA. During a 
    postulated accident, this ventilation system, which does not contain a 
    charcoal filter unit, would draw Enclosure Building air (contaminated 
    with any containment leakage) from the East Penetration Room and 
    discharge it through the 45.8-meter (150-foot) high Unit 2 vent. The 
    lack of a charcoal filter and the lower release point would 
    significantly increase the potential of a thyroid dose in excess of the 
    10 CFR Part 100 guideline at the exclusion area boundary.
        The Technical Specifications for Millstone Unit 2 require that the 
    Enclosure Building integrity be maintained to ensure that the Enclosure 
    Building Ventilation System limits the site boundary doses to within 10 
    CFR Part 100 guidelines following a postulated design basis accident. 
    NRC performed a design basis dose calculation which took into account 
    the lack of charcoal filtration and the lower elevation release path 
    which would result from the noted design deficiency. This calculation 
    indicated that an exclusion area boundary dose to the thyroid greater 
    than the 10 CFR Part 100 guideline of 3000 millisievert (mSv) (300 rem) 
    would occur. It also indicated that the whole body dose would not 
    exceed the 250 mSv (25 rem) 10 CFR Part 100 guideline. The NRC 
    calculation was very conservative in that it assumed that all of the 
    designed allowable containment leakage, following the design basis 
    accident, would be through the penetrations in the East Electrical 
    Penetration Room and released from the Enclosure Building through the 
    Hydrogen Analyzer Ventilation system.
        Cause or Causes--The cause of this condition was an original design 
    deficiency of the hydrogen analyzer cabinet exhaust system.
    
    Actions Taken to Prevent Recurrence
    
        Licensee--The licensee modified the design to route the exhaust 
    path from the hydrogen analyzer cabinet into the enclosure building 
    ventilation system, thereby going through the appropriate filtration, 
    in order to reduce any post-LOCA radioactive release to below 10 CFR 
    Part 100 guidelines. The waste gas sample sink was relocated from the 
    enclosure building to the auxiliary building. This design modification 
    was implemented prior to the start up of Millstone Unit 2.
        NRC--On February 16, 1995, NRC exercised enforcement discretion and 
    did not issue a violation. In accordance with the ``General Statement 
    of Policy and Procedure for NRC Enforcement Actions,'' (Enforcement 
    Policy) then set out at 10 CFR Part 2, Appendix C, this design 
    deficiency would normally be categorized as a Severity Level III 
    violation and enforcement action would normally be considered because 
    it involved a violation of the Technical Specifications and could have 
    resulted in 10 CFR Part 100 guidelines being exceeded in the event of a 
    LOCA. However, the exercise of discretion for the apparent Severity 
    Level III violation 
    
    [[Page 58389]]
    was determined to be warranted in this instance because: (1) The 
    condition was identified by the licensee's staff as a result of a 
    questioning attitude by a system engineer and was promptly reported to 
    the NRC; (2) the condition, which existed since initial startup, was 
    difficult to discover and such identification was not likely by routine 
    inspection, surveillance and quality assurance activities; (3) 
    comprehensive corrective actions were taken within a reasonable time 
    period that involved an adequate root cause determination and a review 
    for failures caused by similar root causes; and (4) the condition was 
    caused by an old performance failure that is not reasonably linked to 
    present performance.
        This event was determined to be plant specific due to the unique 
    design of the ventilation system.
    
    Other NRC Licensees (Industrial Radiographers, Medical Institutions, 
    Industrial Users, etc.)
    
    95-4 Medical Brachytherapy Misadministration at the University of 
    Virginia, in Charlottesville, Virginia
    
        One of the AO reporting guidelines notes that a therapeutic 
    exposure to any part of the body not scheduled to receive radiation can 
    be considered an AO.
        Date and Place--March 14, 1995; University of Virginia Medical 
    Center; Charlottesville, Virginia.
        Nature and Probable Consequences--A patient was prescribed a manual 
    brachytherapy procedure using cesium-137 (Cs-137) sources loaded in an 
    applicator, for a total gynecological treatment dose of 3000 centigray 
    (cGy) (3000 rad).
        During insertion of the applicator into the patient, one of the 
    sources fell onto the patient's bed and was unnoticed by the licensee 
    staff involved in performing the procedure. A nurse found the source in 
    the bed on March 15 and removed it. The source was reloaded into the 
    applicator and the physician revised the prescribed dose to 2500 cGy 
    (2500 rad). The licensee estimated that the source remained at 
    approximately 10 centimeters (4 inches) from the patient's foot for 18 
    hours and delivered a dose of about 13 cGy (13 rad) to the foot.
        The licensee notified the referring physician and the patient of 
    the misadministration. An NRC medical consultant was obtained who 
    concluded that the patient was receiving appropriate follow-up care. In 
    addition, the licensee and the medical consultant concluded that the 
    patient will not experience any adverse health effects as a result of 
    the misadministration.
        Cause or Causes--The licensee's staff involved in the brachytherapy 
    procedure were not familiar with handling of the applicator that 
    contained the Cs-137 sources. Also, because of anatomic characteristics 
    of the patient, the physician had difficulty inserting the source 
    carrier into the applicator. The design of the afterloading device 
    allows the source to slide out of the carrier if any unusual 
    manipulation of source carrier is required. The difficulty experienced 
    by the physician in inserting the source in the applicator and the 
    design of the source carrier resulted in the source falling out of the 
    carrier during the insertion process.
    
    Actions Taken to Prevent Recurrence
    
        Licensee--The licensee provided training for its staff, involved in 
    brachytherapy procedures, concerning the precautions which must be 
    taken when handling an applicator such as the one used in the subject 
    procedure. Also, emphasis was placed on the need to be more attentive 
    during the source insertion process in order to account for all 
    prescribed sources.
        NRC--NRC conducted a special inspection on March 23-24, 1995, to 
    review the circumstances surrounding the misadministration. The 
    inspection report was issued on May 2, 1995. Enforcement action will be 
    taken as appropriate.
    
    95-5  Medical Therapeutic Radiopharmaceutical Misadministration of 
    Iodine-131 at Massachusetts General Hospital in Boston, Massachusetts
    
        One of the AO reporting guidelines notes that administering a 
    therapeutic dose of a radiopharmaceutical differing from the prescribed 
    dose by more than 10 percent and the actual dose is greater than 1.5 
    times the prescribed dose can be considered an AO.
        Date and Place--May 9, 1995; Massachusetts General Hospital; 
    Boston, Massachusetts.
        Nature and Probable Consequences--A patient was prescribed a 296 
    megabecquerel (MBq) (8 millicurie [mCi]) dosage of iodine-131 (I-131) 
    for hyperthyroidism; however, a dosage of 1106.3 MBq (29.9 mCi) was 
    administered.
        Representatives of the hospital informed the referring physician 
    and the patient of the misadministration. An NRC medical consultant was 
    obtained to evaluate the event and stated that the higher dosage given 
    to the patient will result in a more likely achievement of the intended 
    therapeutic goal to eliminate the patient's hyperthyroidism. 
    Additionally, the consultant determined that it is unlikely that the 
    patient is at significant risk of experiencing long-term consequences 
    from receiving the higher dosage beyond the risk associated with the 
    prescribed dosage. Therefore, the impact on the patient's health is 
    expected to be negligible with no expected long-term disability. (The 
    intent of the prescribed dose was to ablate the portion of the thyroid 
    remaining after surgery and then support the patient with thyroid 
    supplement the rest of her life. This did not change with the 
    administered dose.)
        Cause or Causes--The licensee stated that this event occurred 
    because of a human error. The technologist involved in this procedure 
    inadvertently switched the labeled lids on the vial shields containing 
    the I-131 dosages prescribed for different patients. Additionally, the 
    technician failed to check for the correct dosage on the vial label, 
    and the wrong dose was administered to the intended patient.
    
    Actions Taken to Prevent Recurrence
    
        Licensee--The licensee instituted a procedure for checking the vial 
    label before giving a dose. In addition, the licensee is obtaining a 
    second dose calibrator which will be used in the out-patient dosing 
    room of the Thyroid Clinic. Each dose will be re-assayed immediately 
    before the I-131 is administered to the patient, rather than relying on 
    the assay which was performed in the Thyroid Lab before the dose was 
    transported to the out-patient dosing room.
        NRC--NRC performed an inspection on May 12, 1995, to learn about 
    the event and determined that it constituted a misadministration as 
    defined in 10 CFR 35.2. NRC determined that this was an isolated 
    violation of the licensee's Quality Management Program and issued a 
    Notice of Violation at the Severity Level IV on June 26, 1995.
    
    95-6  Multiple Medical Brachytherapy Misadministrations at Madigan Army 
    Medical Center in Fort Lewis, Washington
    
        One of the AO reporting guidelines notes that administering a 
    therapeutic dose from a sealed source such that the treatment dose 
    differs from the prescribed dose by more than 10 percent and the event 
    (regardless of health effects) affects two or more patients at the same 
    facility can be considered an AO.
        Date and Place--February 1994 through May 1995; Madigan Army 
    Medical Center (MAMC); Fort Lewis, Washington. 
    
    [[Page 58390]]
    
        Nature and Probable Consequences--Four patients were prescribed 
    brachytherapy procedures, using iridium-192 seeds of different source 
    strengths, and received doses other than those prescribed because of 
    the same computer input error. (The same computer input error could 
    cause either underdoses or overdoses because the algorithm used was 
    dose dependent.) Details of the misadministrations are as follows:
        Patient A: The patient was prescribed a dose of 2800 centigray 
    (cGy) (2800 rad) for a gynecological brachytherapy treatment, but 
    received a dose of about 1680 cGy (1680 rad) instead.
        Patient B: Event 1--The patient was prescribed a dose of 1600 cGy 
    (1600 rad) for lung treatment, but received a dose of about 2128 cGy 
    (2128 rad) instead.
        Event 2--On another day, the same patient was prescribed a dose of 
    1500 cGy (1500 rad) for lung treatment, but received a dose of about 
    2350 cGy (2350 rad) instead.
        Patient C: The patient was prescribed a dose of 3000 cGy (3000 rad) 
    for gynecological treatment, but received a dose of about 5142 cGy 
    (5142 rad) instead.
        Patient D: The patient was prescribed a dose of 1500 cGy (1500 rad) 
    for a biliary tract treatment, but received a dose of about 2050 cGy 
    (2050 rad) instead.
        The licensee does not expect the patients to experience any adverse 
    health effects as a result of the misadministrations.
        Cause or Causes--Based upon NRC's initial review of the 
    misadministrations, it appears that the probable causes of the 
    treatment errors were failures to: (1) independently review or check 
    the data input to the computerized treatment planning system, and (2) 
    perform an independent check of dose rate calculations generated by the 
    treatment planning system.
    
    Actions Taken to Prevent Recurrence
    
        Licensee--The physics staff at MAMC promptly corrected the data 
    entered into the computer treatment planning computer, recalculated the 
    doses received by the patients, and took steps to ensure that 
    appropriate data will be used for future treatment plans.
        NRC--NRC initiated an inspection on June 6, 1995, to review the 
    circumstances associated with the misadministrations and to review the 
    licensee's corrective actions. (As of the date of this report, the 
    inspection is ongoing.) An NRC medical consultant will review each case 
    in order to provide an independent assessment of the potential 
    consequences of the overdoses.
    
        Dated at Rockville, MD this 20th day of November, 1995.
    
        For the Nuclear Regulatory Commission.
    John C. Hoyle,
    Secretary of the Commission.
    [FR Doc. 95-28835 Filed 11-24-95; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Published:
11/27/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Action:
(1) Chain locked the isolation valve in the RHR-RWST connecting line, and made the plant manager and operations manager solely responsible for access to this valve; (2) removed the use of the RHR-RWST connecting line from the RHR boration procedures; and (3) approached the Westinghouse Owners
Document Number:
95-28835
Pages:
58387-58390 (4 pages)
PDF File:
95-28835.pdf