97-29138. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 214 (Wednesday, November 5, 1997)]
    [Notices]
    [Pages 59912-59927]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-29138]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from October 10, 1997, through October 24, 1997. 
    The last biweekly notice was published on October 22, 1997 (62 FR 
    54866).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and should cite the publication date and 
    page number of this Federal Register notice. Written comments may also 
    be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, MD from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By December 5, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for
    
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    leave to intervene or who has been admitted as a party may amend the 
    petition without requesting leave of the Board up to 15 days prior to 
    the first prehearing conference scheduled in the proceeding, but such 
    an amended petition must satisfy the specificity requirements described 
    above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket No. 50-317, Calvert Cliffs 
    Nuclear Power Plant, Unit No. 1, Calvert County, MD
    
        Date of amendment request: October 2, 1997.
        Description of amendment request: The amendment request would 
    change the Technical Specifications to identify a proposed upgrade of 
    the electrical capacity of the No. 1B emergency diesel generator.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The Engineered Safety Features (ESF) electrical system provides a 
    reliable source of electrical power to the 4.16 kV ESF busses to 
    operate the necessary accident mitigation equipment, should offsite 
    power be lost. The proposed change to the Technical Specifications was 
    prompted by the upgrade of the electrical and mechanical capacity of 
    the No. 1B Fairbanks Morse Emergency Diesel Generator (EDG). The 
    increased electrical capacity of the No. 1B Fairbanks Morse EDG will 
    give the operators greater flexibility in the choice of discretionary 
    loads for the mitigation of accidents. This modification necessitates 
    changes to the Technical Specifications.
        The ESF electrical system, including the four EDGs, is used to 
    mitigate the consequences of an accident. The modification to upgrade 
    the capacity of No. 1B EDG will increase the electrical output of the 
    EDG, but will not change the configuration of the ESF electrical system 
    or any support systems such that the EDGs would become an accident 
    initiator. Therefore, the proposed change would not increase the 
    probability of an accident previously evaluated.
        The proposed Technical Specifications will continue to demonstrate 
    the reliability and capability of the upgraded No. 1B EDG to perform 
    its accident mitigation function. The proposed changes to the 
    surveillance requirements do not alter the intent or performance of the 
    surveillance. Only the electrical loadings changed, reflecting the 
    change in the EDG's electrical capacity. Implementation of the proposed 
    Technical Specifications will not reduce the ability of No. 1B EDG to 
    perform its safety functions. Any auxiliary systems that required 
    modification or analysis to support the upgraded ratings of the 1B 
    Fairbanks Morse EDG have been determined not to adversely impact 
    operation of any other plant systems necessary to mitigate the 
    consequences of an accident. Therefore, the proposed change would not 
    increase the consequences of an accident previously evaluated.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. Would not create the possibility of a new or different type of 
    accident from any accident previously evaluated.
        The proposed change increases the electrical loading for 
    surveillance requirements to reflect the upgrade to the electrical 
    capacity of the No. 1B Fairbanks Morse EDG. This change does not add 
    any new equipment, modify any interfaces with any existing equipment, 
    change the equipment's function, or the method of operating the 
    equipment to be modified. The system will continue to operate in the 
    same manner as before the capacity upgrades were implemented. The 
    modified No. 1B EDG will continue to function as an accident
    
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    mitigator, and will not become an initiator of any accident.
        Therefore, the proposed change does not create the possibility of a 
    new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of safety.
        The safety function of the EDG is to provide a reliable source of 
    electrical power to the ESF electrical system sufficient to power the 
    necessary accident mitigation equipment, should offsite power be lost. 
    This safety function is demonstrated by performing the required 
    surveillance tests. The proposed changes do not alter the intent or 
    method of performance of any of the surveillance tests.
        The proposed change to the Technical Specifications was prompted by 
    the upgrade of the electrical and mechanical capacity of the No. 1B 
    Fairbanks Morse EDG. The higher electrical capacity will result in an 
    increase in the margin between No. 1B EDG's electrical capacities and 
    the electrical power required to operate safety-related equipment 
    required for safe shutdown or accident mitigation. The increased 
    electrical capacity results in the need to increase the electrical 
    loadings used in the surveillance tests. The changes in the 
    surveillance tests will continue to ensure that the EDG is tested 
    appropriately and will continue to perform its safety function. In 
    addition, it should be noted that upgrades on identical Fairbanks Morse 
    EDGs have already been performed on Unit 2 and have resulted in 
    identical changes to the Unit 2 Technical Specifications. Because of 
    the increased electrical margin afforded by the upgraded EDG, these 
    modifications may be considered an increase in the margin of safety.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, MD 20678.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IL; Docket Nos. STN 50-
    456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will County, 
    IL
    
        Date of amendment request: September 8, 1997.
        Description of amendment request: The proposed amendment would 
    revise Byron and Braidwood Technical Specification (TS) 4.5.2.b and 
    associated bases as they relate to the requirement to vent the 
    Emergency Core Cooling System (ECCS) pump casings and discharge piping 
    high points outside containment. The change will revise the Unit 1 
    requirement for ultrasonic examinations every 31 days to also include 
    ultrasonic examination of the piping at the 1CV206 valve for Byron 
    (1CV207 valve for Braidwood) if the 1B Chemical and Volume Control (CV) 
    pump is idle. These changes are required to align the surveillance 
    requirements for Unit 1 with those of Unit 2. In addition, the 
    condition that the Unit 1 requirements will be applicable only until 
    the end of the current cycle is deleted consistent with the Unit 2 
    requirements. With these changes there will no longer be the need to 
    maintain separate pages for Unit 1 and Unit 2 requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes will align the surveillance requirements for 
    both Units 1 and 2 with the installed system design and normal 
    operating conditions. No increase in the probability of an accident 
    will occur as a result of this change. The conduct of surveillances 
    required by the Technical Specifications is not postulated to initiate 
    an accident. The level of surveillance performed to date has provided 
    confidence that the objective of the current surveillance requirement 
    has been met. As such, the proposed change does not result in a 
    significant increase in the probability of occurrence of a previously 
    analyzed accident.
        The consequences of a previously analyzed accident are not 
    increased. Operating experience has shown that the level of 
    surveillance performed to date is sufficient to provide confidence that 
    no significant voiding has occurred in the affected piping. Ultrasonic 
    examinations have confirmed the water solid condition of the piping. 
    Although voiding is not expected, evaluation of postulated voided 
    conditions confirm that unacceptable dynamic loading would not occur, 
    and, therefore, the integrity of the ECCS piping is not compromised. 
    Thus, the ECCS will be capable of performing its design function of 
    cooling the reactor core and providing shutdown capability following 
    initiation of the certain accidents. This will ensure that the 
    consequences of a previously analyzed accident are not significantly 
    increased.
        Therefore, these proposed revisions do not result in a significant 
    increase in the probability or consequences of an accident previously 
    analyzed.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not create the possibility of a new or 
    different kind of accident. ComEd has evaluated the piping 
    configuration for the ECCS discharge piping of the ECCS subsystems. A 
    specific engineering evaluation of both a voided 2-inch and 8-inch RH 
    [Residual Heat Removal] line was performed. This evaluation concluded 
    that the piping can withstand the dynamic loads caused by the maximum 
    credible air void. Due to the higher-pressure rating and smaller size 
    of the SI [Safety Injection] and CV discharge piping, this evaluation 
    is considered bounding for the ECCS subsystems. The results of the 
    evaluation were submitted for staff review in a letter dated March 12, 
    1990, in support of Amendments 47 and 36 to the Operating Licenses for 
    Byron and Braidwood, respectively. The proposed changes will not result 
    in new failure modes because no new equipment is installed, and 
    installed equipment is not operated in a new or different manner. 
    Manual venting operations have been performed as permitted by system 
    operation and piping configuration. This venting surveillance does not 
    apply to subsystems in communication with operating systems because the 
    flows and/or pressures prevalent in these systems are sufficient to 
    provide confidence that water hammer which could occur from voiding 
    would not result in unacceptable dynamic loads from water hammer will 
    not occur. Accordingly, this change will not create the possibility of 
    a new or different kind of accident.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
    
    [[Page 59915]]
    
        The margin of safety is not significantly reduced because the 
    proposed change will provide sufficient assurance that excessive 
    voiding will not occur. This will assure proper system functioning. 
    Venting of the idle subsystems, in conjunction with the operating 
    conditions of the subsystems in operation, provides confidence that 
    voiding is not present. This has been confirmed by the performance of 
    ultrasonic examinations of the piping of interest. This meets the 
    objective of the surveillance requirement and thus preserves the margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, IL 61010; for 
    Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, IL 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, IL 60603.
        NRC Project Director: Robert A. Capra.
    
    Consumers Energy Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, MI
    
        Date of amendment request: January 18, 1996, as revised October 1, 
    1997.
        Description of amendment request: The original proposed amendment 
    (January 18, 1996) would have deleted the requirement in Section 6.5.6 
    of the Technical Specifications (TS) to perform inservice inspections 
    of the primary coolant pump (PCP) flywheels. The October 1, 1997, 
    submittal would revise Section 6.5.6 of the TS to lengthen the flywheel 
    inspection period to 10 years rather than delete it entirely. The note 
    added by Amendment 175 for the deletion of the inspection at the end of 
    Cycle 12 would also be deleted. The original submittal was previously 
    noticed in the Federal Register on September 11, 1996 (61 FR 47976).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee provided 
    its analysis of the issue of no significant hazards consideration in 
    its original submittal. In its revised submittal the licensee stated 
    that the conclusions reached in the original no significant hazards 
    consideration determination were still valid because the revised 
    submittal just reduces the frequency of the test as opposed to deleting 
    it. The original no significant hazards consideration discussion is 
    presented below:
        The following evaluation supports the finding that operation of the 
    facility in accordance with the proposed change to the Technical 
    Specifications would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to the Technical Specifications would delete 
    the requirement to perform non-destructive examination of the upper 
    flywheel on the PCPs. The fracture mechanics analyses conducted to 
    support the change show that a preexisting crack sized just below 
    detection level will not grow to the flaw size necessary to result in 
    flywheel failure within the life of the plant. This analysis 
    conservatively assumes minimum material properties, maximum flywheel 
    accident speed, location of the flaw in the highest stress area and a 
    number of startup/shutdown cycles eight times greater than expected. 
    Since an existing flaw in the flywheel will not grow to the allowable 
    flaw size under normal operating conditions or to the critical flaw 
    size under LOCA [loss-of-coolant accident] conditions over the life of 
    the plant, elimination of inservice inspection for such cracks during 
    the plant's life will not involve a significant increase in the 
    probability of an accident previously considered.
        The proposed changes do not increase the amount of radioactive 
    material available for release or modify any systems used for 
    mitigation of such releases during accident conditions. Therefore, 
    operation of the facility in accordance with the proposed change to the 
    Technical Specifications would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed change to the Technical Specifications would not 
    change the design, configuration, or method of operation of the plant 
    and therefore, operation of the facility in accordance with the 
    proposed change to the Technical Specifications would not create the 
    possibility of a new or different kind of accident from any previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to the Technical Specifications would not 
    result in a significant reduction in the margin of safety. Significant 
    conservatisms have been used for calculating the allowable flaw size, 
    critical flaw size and crack growth rate in the PCP flywheels. These 
    include minimum material properties, maximum flywheel accident speed, 
    location of the postulated flaw in highest stress area and a number of 
    startup/shutdown cycles eight times greater than expected. Since an 
    existing flaw in the flywheel will not grow to the maximum allowable 
    flaw size under normal operating conditions or to the critical flaw 
    size under LOCA conditions over the life of the plant, elimination of 
    inservice inspections for such cracks during the plant's life will not 
    involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. In addition, the staff agrees that this analysis bounds the 
    conditions in the revised submittal. The editorial change to delete an 
    obsolete note has no effect on plant operation or safety and also 
    satisfies the three standards of 10 CFR 50.92(c). Therefore, the NRC 
    staff proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, MI 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Energy 
    Company, 212 West Michigan Avenue, Jackson, MI 49201.
        NRC Project Director: John N. Hannon.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, NJ
    
        Date of amendment request: October 10, 1997.
        Description of amendment request: The proposed change (TSCR 253) 
    would reflect the registered trade name of ``GPU Nuclear'' in the 
    operating license for the Oyster Creek Nuclear Generating Station 
    (OCNGS) and change the legal name of the operator of OCNGS from GPU 
    Nuclear Corporation to GPU Nuclear, Inc. In addition, two minor 
    editorial corrections are included.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the facility in accordance with the proposed amendment 
    would not involve a significant increase in the probability of 
    occurrence or the consequences of an accident previously evaluated. The 
    proposed amendment adds to the license and the technical specifications 
    the trade name of the
    
    [[Page 59916]]
    
    Owner of Oyster Creek. The change in the legal name of the operator of 
    Oyster Creek is an administrative change made to reflect the name 
    changes made throughout the GPU family of companies. The name change 
    has no impact on plant design or operation.
        Operation of the facility in accordance with the proposed amendment 
    would not create the possibility of a new or different kind of accident 
    from any accident previously evaluated because no new failure modes are 
    created by the proposed changes. The use of a trade name for the Owner 
    of Oyster Creek and the change in the legal name of the operator of 
    Oyster Creek has no impact on plant design or operation. Thus, there is 
    no creation of the possibility of a new or different kind of accident 
    from those previously evaluated.
        Operation of the facility in accordance with the proposed amendment 
    will not involve a significant reduction in a margin of safety. The 
    proposed amendment does not change any operating limits for reactor 
    operation.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. In addition, the staff has reviewed the licensee's proposed 
    editorial changes and determined that they do not effect the 
    conclusions of the analysis. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ronald B. Eaton, Acting Director.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 1, Oswego County, NY
    
        Date of amendment request: October 21, 1997. This notice supersedes 
    a previous notice, (62 FR 30625), published June 4, 1997, which was 
    based upon the licensee's application for amendment dated May 16, 1997. 
    The licensee's application dated October 21, 1997, supersedes the May 
    16, 1997, submittal in its entirety.
        Description of amendment request: The proposed amendment would 
    change the administrative section of the Technical Specifications (TS) 
    regarding the Operations organization. Specifically, TS 6.2.2i 
    currently states that ``The Manager Operations, Station Shift 
    Supervisor Nuclear and Assistant Station Shift Supervisor Nuclear shall 
    hold senior reactor operator licenses.'' This would be changed to state 
    ``As a minimum, either the Manager Operations or the General Supervisor 
    Operations shall hold a senior reactor operator license. The Station 
    Shift Supervisor Nuclear and Assistant Station Shift Supervisor Nuclear 
    shall hold senior reactor operator licenses.'' In addition TS 6.3.1 
    would be revised to indicate an additional exception to the operating 
    staff's qualification requirements set forth in American National 
    Standard Institute (ANSI) N18.1-1971, ``Selection and Training of 
    Nuclear Power Plant Personnel.'' Specifically, this change would 
    require that the Manager Operation, in lieu of meeting the senior 
    reactor operator (SRO) requirements of ANSI N18.1-1971, shall (1) hold 
    an SRO license at the time of appointment, or (2) have held an SRO 
    license at Nine Mile Point Nuclear Station Unit 1 or a similar unit, or 
    (3) have been certified for equivalent SRO knowledge.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Nine Mile Point Unit 1 [NMP1], in accordance 
    with the proposed amendment, will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The addition of the position of GSO and the requirement for either 
    the GSO or the Manager Operations to have an SRO license is a 
    restructuring of the Operations department. The proposed changes are 
    administrative changes that provide additional Operations management 
    oversight capabilities. Additional restrictions placed on the Manager 
    Operations minimum qualification requirements for experience and SRO 
    level knowledge for the resulting organization meet the intent of ANSI 
    N18.1-1971 and SRP [Standard Review Plan, NUREG-0800] 13.1.1-13.1.3. No 
    physical modification of the plant is involved and no changes to the 
    methods in which plant systems are operated are required.
        None of the precursors of previously evaluated accidents are 
    affected, and no new failure modes are introduced. Therefore, this 
    change will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The addition of the position of GSO and the requirement for either 
    the GSO or the Manager Operations to have an SRO license is a 
    restructuring of the Operations department. The proposed changes are 
    administrative changes that provide additional Operations management 
    oversight capabilities. Additional restrictions placed on the Manager 
    Operations minimum qualification requirements for experience and SRO 
    level knowledge ensure the resulting organization meets the intent of 
    ANSI N18.1-1971 and SRP 13.1.1-13.1.3. No physical modification of the 
    plant is involved and no changes to the methods in which plant systems 
    are operated are required. As such, the change does not introduce any 
    new failure modes or conditions that may create a new or different 
    accident. Therefore, this change does not itself create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The addition of the position of GSO and the requirement for either 
    the GSO or the Manager Operations to have an SRO license is a 
    restructuring of the Operations department. The proposed changes are 
    administrative changes that provide additional Operations management 
    oversight capabilities. Additional restrictions placed on the Manager 
    Operations minimum qualification requirements for experience and SRO 
    level knowledge ensure the resulting organization meets the intent of 
    ANSI N18.1-1971 and SRP 13.1.1-13.1.3. No physical modification of the 
    plant is involved and no changes to the methods in which plant systems 
    are operated are required. As such, this change does not in itself 
    adversely affect any physical barrier to the release of radiation to 
    plant personnel or to the public. Therefore, the change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
    [[Page 59917]]
    
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, NY 
    13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa.
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, CT
    
        Date of amendment request: October 7, 1997.
        Description of amendment request: Technical Specifications 4.6.1.1, 
    3/4.6.1.2, and 3/4.6.1.3 require the testing of the containment to 
    verify leakage limits at a specified test pressure. The proposed 
    amendment would (1) modify the list of valves that can be opened in 
    Modes 1 through 4, (2) remove a footnote on Type A testing, and (3) 
    make editorial changes to the Technical Specifications and associated 
    Bases sections.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 10 CFR 
    50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this conclusion 
    is that the three criteria of 10 CFR 50.92(c) are not satisfied. The 
    proposed revision does not involve [an] SHC because the revision would 
    not:
        1. Involve a significant increase in the probability or consequence 
    of an accident previously evaluated.
        The proposed change to Technical Specification Surveillance 4.6.1.1 
    deletes valves from the list of containment isolation valves that may 
    be opened under administrative control. Deleting the valves, which 
    means that they are not allowed to be opened under the Limiting 
    Condition of Operation, [cannot] cause an accident. The valves being 
    added in the steam lines to the steam-driven auxiliary feedwater pump 
    can be used to heat the steam lines prior to testing the steam-driven 
    auxiliary feed water pump. Heating the steam lines prior to testing the 
    steam-driven auxiliary feedwater pump does not increase the likelihood 
    of a steam line break.
        The administrative change of replacing the ``-'' with an ``*'' in 
    the valve designation can neither cause [an] accident nor affect the 
    consequences of any accident.
        The addition of the RHR [residual heat removal] system containment 
    isolation valves reflects the fact that these valves can be opened 
    during Mode 4 to allow plant heatup and cooldown. Plant heatup and 
    cooldown, in accordance with normal plant operation and the Technical 
    Specifications, does not increase the likelihood of the above 
    accidents.
        The administrative controls include the appropriate considerations 
    that containment integrity will be established, when required. By 
    establishing containment integrity, the assumptions in the design basis 
    analyses are assured. This means that for LOCA [loss-of-coolant 
    accident], steam line break and feed line break accidents inside 
    containment, there is no effect on their consequences.
        Valves in the steam lines to the steam-driven auxiliary feedwater 
    pump are being added to the list of valves allowed to be opened under 
    administrative control. This means that these could be open at the 
    initiation of an accident. The administrative controls under which 
    these valves are opened provides assurance that containment integrity 
    will be established, when required. Similarly, for an SGTR [steam 
    generator tube rupture], Locked Rotor or Control Rod Ejection event, 
    the administrative controls provides assurance that these valves will 
    be closed and, therefore, allowing them to be opened will not adversely 
    impact the consequences of these events. If failure to close is 
    postulated as a single failure for these events, the results would be 
    bounded by the analyses described in the FSAR [final safety analysis 
    report]. For example, the Locked Rotor accident assumes a stuck open 
    steam generator power-operated pressure relief valve (SG PORV). The 
    steam released by the assumed single failure of the SG PORV, for the 
    twenty minutes until the valve is isolated, would exceed the expected 
    releases as a result of failure to close valve 3MSS*V885, 3MSS*V886, or 
    3MSS*V887, which are in \1/4\ inch lines. Therefore, allowing these 
    valves to be opened under administrative control does not effect the 
    consequences of the previously evaluated accidents.
        The FSAR, Section 15.1.5, provides the assumptions on steam 
    releases for the consequences of the steam line break accident. The 
    steam generator with the broken steam line is assumed to be open to the 
    atmosphere for the duration of the event and, therefore, these valves 
    being open would not impact that assumption. For the unaffected steam 
    generators, steam is assumed released to the atmosphere to remove decay 
    heat. These valves are in \1/4\ inch lines which means that any steam 
    released via this path would only be a small fraction of decay heat and 
    will not adversely affect control of decay heat removal. Therefore, 
    whether these valves are open or not will not affect the consequences 
    of a steam line break outside containment.
        Allowing the RHR system containment isolation valves to be open, 
    under administrative control in Mode 4, does not change the way the 
    system is operated. This proposed change to the footnote does not 
    change the operators response to an accident in Mode 4. Therefore, the 
    addition of these valves does not affect the consequences of the 
    previously evaluated accidents.
        The proposed change to Technical Specification Surveillance 
    4.6.1.2.a will delete footnote ``*'' which referred to an exemption 
    granted by the NRC to permit the Type A test to be delayed until RFO6 
    [refueling outage 6]. However, the current extended shutdown has 
    significantly delayed RFO6 and NNECO intends to perform the Type A test 
    during this midcycle shutdown. The deletion of the footnote does not 
    alter the operation of any system or the containment or containment 
    airlocks, as assumed for accident analyses.
        Additionally, Technical Specifications 4.6.1.1, 3/4.6.1.2, and 3/
    4.6.1.3, and Bases Sections 3/4.6.1.1, 3/4.6.1.2, and 3/4.6.1.3 are 
    reworded to provide clarity and consistency. These proposed changes do 
    not alter the operation of any system or the containment or containment 
    airlocks during accident analyses.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to Technical Specifications 4.6.1.1, 3/
    4.6.1.2, and 3/4.6.1.3 and Bases Sections 3/4.6.1.1, 3/4.6.1.2, and 3/
    4.6.1.3 do not alter the operation of any system or the containment or 
    containment airlocks, during normal operation or as assumed in accident 
    analyses.
        Deleting containment isolation valves from the list of those that 
    are allowed to be opened under administrative control can not modify 
    plant response to an accident. Adding administrative control when the 
    RHR system containment isolation valves are opened in Mode 4 for normal 
    plant cooldown and heatup can not create a new or different accident. 
    Allowing valves to be opened
    
    [[Page 59918]]
    
    to heat the steam lines to the steam-driven auxiliary feedwater pump 
    prior to testing does not create the possibility of a new or different 
    accident. The administrative change to the valve designation can not 
    modify plant response.
        Therefore, the proposed revision does not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to Technical Specifications 4.6.1.1, 3/
    4.6.1.2, and 3/4.6.1.3, and Bases Sections 3/4.6.1.1, 3/4.6.1.2, and 3/
    4.6.1.3 do not alter the design, maintenance or function of any system 
    or the containment or the containment airlocks. Additionally, the 
    proposed changes do not alter the testing of any system or the 
    containment or containment airlocks, or alter any assumption used in 
    the accident analyses.
        The considerations associated with administrative control are being 
    added to the bases of the technical specification. These considerations 
    are identical to those provided in GL 91-08 [Generic Letter 91-08]. 
    This means that the changes will maintain the margin of safety. The 
    valves that are allowed to be open in the steam lines to the steam-
    driven auxiliary feedwater [pump] do not impact the accident analyses 
    and therefore do not reduce the margin of safety. The addition of the 
    RHR system containment isolation valves reflects the fact that these 
    valves are opened for heatup and cooldown in Mode 4. The change adds 
    the requirements of administrative controls to these RHR system valves 
    in Mode 4, but does not modify the use of these valves. The 
    administrative change to the valve designation can not affect the 
    margin of safety.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is determined 
    that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT, and the Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT.
        NRC Deputy Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, CT
    
        Date of amendment request: October 15, 1997.
        Description of amendment request: Technical Specification 
    Surveillances 4.1.2.3.1, 4.1.2.4.1, 4.5.2, 4.6.2.1, and 4.6.2.2 require 
    the recirculation spray, quench spray, residual heat removal, 
    centrifugal charging, and safety injection pumps to be tested on a 
    periodic basis and after modifications that alter subsystem flow 
    characteristics. The proposed changes to these surveillances would 
    include replacing the specific surveillance pump pressure with a 
    statement that the test be conducted in accordance with Specification 
    4.0.5, Inservice Testing Program. The proposed changes would also 
    include a decrease in the required individual safety injection and 
    centrifugal charging pump injection line flow rates, an increase in the 
    allowed individual safety injection pump runout flow rate, and 
    editorial changes to the surveillances.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 10 CFR 
    50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this conclusion 
    is that the three criteria of 10 CFR 50.92(c) are not satisfied. The 
    proposed revision does not involve an SHC because the revision would 
    not:
        1. Involve a significant increase in the probability or consequence 
    of an accident previously evaluated.
        The Technical Specification changes transfer control of the pump 
    developed head requirements for the Centrifugal Charging, Safety 
    Injection, Quench Spray, Residual Heat Removal, and Recirculation Spray 
    pumps from the Technical Specifications to the Inservice Test program. 
    The acceptance criteria will still assure that the safety analysis 
    assumptions are valid. The Technical Specification changes reduce the 
    minimum flow requirements for the Charging and Safety Injection pumps 
    and increase the maximum allowed flow for the Safety Injection pumps. 
    Modifying the surveillance requirements [cannot] cause an accident and, 
    therefore, [cannot] increase the probability of an accident. The 
    revised minimum required flows are consistent with the flows used in 
    the accident analyses and, therefore, the change [cannot] increase the 
    consequences of any accident. The safety injection pumps are disabled 
    such that they [cannot] be a source of mass addition to the RCS 
    [reactor coolant system] whenever the cold overpressure system is 
    required to be operable. Therefore, the increase in the allowed maximum 
    safety injection pump flow has no effect on the cold overpressure 
    accident analysis.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes transfer control of the pump developed head 
    requirements from the Technical Specifications to the Inservice Test 
    program and modify the required flow surveillance values. The 
    surveillance values that are used in the Inservice Test program and the 
    Technical Specification are consistent with the accident analysis. The 
    increase in the allowed maximum safety injection pump flow does not 
    impact the cold overpressure accident analysis. The changes do not 
    involve any changes to the way that the pumps are operated. The pumps 
    will be used post-accident the same way as they are used prior to the 
    change.
        Therefore, the proposed revision does not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The control of the pump developed head acceptance criteria is being 
    transferred from the Technical Specification to the Inservice Test 
    program. The acceptance criteria, at a minimum, will assure that the 
    design basis analyses are valid. The minimum pump flow surveillance 
    requirements in Specification 4.5.2.h are consistent with the 
    assumptions of the accident analysis. The maximum allowed Safety 
    Injection flow does not exceed the vendor recommendation for maximum 
    continuous runout flow. The NPSH [net positive suction head] available 
    to the pumps during both the injection and recirculation phases post-
    accident
    
    [[Page 59919]]
    
    exceeds the NPSH required at the higher allowed flow. Also, the safety 
    injection pumps are disabled so that they [cannot] be an injection 
    source when the cold overpressure system is required to be operable 
    which means that the increase in maximum flow does not affect the cold 
    overpressure accident analysis. Restricting orifices are being 
    installed in the injection lines from the safety injection and charging 
    pumps to the Reactor Coolant System as required. The restricting 
    orifices and the changes to the required flows will allow for resetting 
    the throttle position of the existing throttle valves. The sizing of 
    the restricting orifices and the associated re-throttling of the 
    throttle valves will be in accordance with Regulatory Guide 1.82. The 
    proposed changes allow for the setting of the throttle valve positions 
    so that the openings will be larger than the sump screen mesh opening 
    size while assuring that the design basis flow values are valid.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is determined 
    that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT, and the Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, NE
    
        Date of amendment request: July 25, 1997.
        Description of amendment request: The proposed amendment request 
    would revise the Technical Specifications (TS) to implement 10 CFR Part 
    50 Appendix J, Option B by referring to Regulatory Guide 1.163, 
    ``Performance-Based Containment Leakage-Test Program,'' with certain 
    exceptions detailed in the licensee's application. This revision 
    supersedes the staff's description of amendment request that was 
    published on October 8, 1997 (62 FR 52586).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change implements Option B of 10 CFR Part 50 Appendix 
    J on performance-based containment leakage testing. The proposed change 
    does not involve a change to the plant design or operation. As a 
    result, the proposed change does not affect any parameters or 
    conditions that contribute to the initiation of any accidents 
    previously evaluated. The proposed change potentially affects the leak-
    tight integrity of the containment structure designed to mitigate the 
    consequences of a Loss-of-Coolant Accident (LOCA). The function of the 
    containment is to maintain functional integrity during and following 
    the peak transient pressures and temperatures and limit fission product 
    leakage following the design basis LOCA. Because the proposed change 
    does not alter the plant design, only the frequency of measuring Type 
    A, B, and C leakage, the proposed change does not directly result in an 
    increase in containment leakage.
        Test intervals will be established based on the performance history 
    of components being tested. The frequency of monitoring the relatively 
    few containment isolation valves and/or containment penetrations 
    subject to above normal leakage will not decrease by implementing 
    Option B of Appendix J. A performance based program will identify those 
    valves and penetrations which must continue to be tested each refueling 
    outage.
        The risk resulting from the proposed changes is characterized as 
    follows, based primarily on the results contained in NUREG-1493 
    ``Performance-Based Containment Leakage Test Program,'' the principal 
    Technical Support Document used by the NRC as the basis for the 
    Appendix J Final Rule:
    Type A Testing
        NUREG-1493 found that the effect of containment leakage on overall 
    accident risk is minimal since risk is dominated by accident sequences 
    that result in failure or bypass of the containment. Industry wide, 
    Integrated Leak Rate Tests (ILRTs) have only found a small fraction of 
    the leaks that exceed current acceptance criteria. Only three percent 
    of all leaks are detectable only by ILRTs, and therefore, by extending 
    the Type A testing intervals, only three percent of all leaks have a 
    potential for remaining undetected for longer periods of time. In 
    addition, when leakage has been detected by ILRTs, the leakage rate has 
    been only marginally above existing requirements. The Fort Calhoun 
    Station Unit No. 1 Type A testing confirms the industry-wide experience 
    that a majority of the leakage experienced during Type A testing is 
    through components tested by Type B and C tests.
        NUREG-1493 found that these observations, together with the 
    insensitivity of reactor accident risk to the containment leakage rate, 
    show that increasing the Type A leakage test intervals would have a 
    minimal impact on public risk.
    Type B and C Testing
        NUREG-1493 found that while Type B and C tests can identify the 
    vast majority (greater than 95 percent) of all potential leakage paths, 
    performance-based alternatives to current local leakage-testing 
    requirements are feasible without significant risk impacts. The risk 
    model used in NUREG-1493 suggests that the number of components tested 
    would be reduced by about 60 percent with less than a three-fold 
    increase in the incremental risk due to containment leakage. Since, 
    under existing requirements, leakage contributes less than 0.1 percent 
    of overall accident risk, the overall impact is very small. In 
    addition, the NRC's Final Regulatory Impact Analysis concluded that 
    while the extended testing intervals for Type B and C tests led to 
    minor increases in potential offsite dose consequences, the beneficial 
    expected decrease in onsite worker dose received during ILRT and local 
    leak rate testing exceeds (by at least an order of magnitude) the 
    potential off-site dose consequences.
        Therefore, the proposed change will not result in a significant 
    increase in the probability or consequences of any accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        There will be no physical alterations to the plant configuration, 
    changes to setpoint values, or changes to the implementation of 
    setpoints or limits as a result of this proposed change. As a result, 
    the proposed change does not affect any of the parameters or conditions 
    that could contribute to initiation of any accidents.
    
    [[Page 59920]]
    
        This change involves the reduction of Type A, B, and C test 
    frequency. Except for the method of defining the test frequency, the 
    methods for performing the actual tests are not changed. No new 
    accident modes are created by extending the testing intervals. No 
    safety-related equipment or safety functions are altered as a result of 
    this change. Extending the test frequency has no influence on, nor does 
    it contribute to, the possibility of a new or different kind of 
    accident or malfunction from those previously analyzed. Therefore, the 
    proposed change does not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed change only affects the frequency of Type A, B, and C 
    testing. Except for the method of defining the test frequency, the 
    methods for performing the actual tests are not changed.
        The frequency of monitoring the relatively few containment 
    isolation valves and/or containment penetrations subject to above 
    normal leakage will not decrease by implementing Option B of Appendix 
    J. A performance based program will identify those valves and 
    penetrations which must continue to be tested each refueling outage. 
    NUREG-1493 has determined that, under several different accident 
    scenarios, the increased risk of radioactivity release from containment 
    is negligible with the implementation of these proposed changes.
        The margin of safety that has the potential of being impacted by 
    the proposed change involves the offsite dose consequences of 
    postulated accidents which are directly related to containment leakage 
    rate. The containment isolation system is designed to limit leakage to 
    La, which is stated in the Fort Calhoun Station Unit No. 1 Technical 
    Specifications to be 0.1 percent by weight of the containment air per 
    24 hours at 60 psig.
        The limitation on containment leakage rate is designed to ensure 
    that total leakage volume will not exceed the value assumed in the 
    accident analyses at the peak accident pressure. The margin to safety 
    for the offsite dose consequences of postulated accidents directly 
    related to the containment leakage rate is maintained by meeting the 
    1.0 La acceptance criteria. The La value is not being modified by this 
    proposed change.
        Except for the method of defining the test frequency, no change in 
    the method of testing is being proposed. The Type B and C tests will 
    continue to be done at 60 psig or greater. Other programs are in place 
    to ensure that proper maintenance and repairs are performed during the 
    service life of the primary containment and systems and components 
    penetrating the primary containment.
        Therefore, the proposed change will not result in a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, NE 68102.
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, NY
    
        Date of amendment request: September 3, 1997.
        Description of amendment request: The proposed amendment would 
    change the Technical Specifications (TSs) to revise the number of hours 
    operating personnel can work in a normal shift. The proposed amendment 
    also contains some administrative changes to the TSs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated?
        A. Establishing operating personnel work hours at, ``an 8 to 12 
    hour day, nominal 40 hour week,'' allows normal plant operations to be 
    managed more effectively and does not adversely effect performance of 
    operating personnel. Overtime remains controlled by site administrative 
    procedures in accordance with NRC Policy Statement on working hours 
    (Generic Letter 82-12). If 8 hour shifts are maintained in part or 
    whole, then acceptable levels of performance from operating personnel 
    is assured through effective control of shift turnovers and plant 
    activities. No physical plant modifications are involved and none of 
    the precursors of previously evaluated accidents are affected. 
    Therefore, this change will not involve a significant increase in the 
    probability or consequence of an accident previously evaluated.
        B. Editorial changes clarify section 6.2.2.g without changing the 
    intent or meaning. The proposed change meets the intent of the NRC 
    Policy Statement on working hours (Generic Letter 82-12).
        C. Changes to sections 3.10.6.1.a and 3.10.9 do not change the 
    intent or meaning of the technical specification sections. 
    Clarification to the table notation in section 4.1 related to the 
    definition of shift checks to monitor plant conditions will continue as 
    intended but are allowed to increase up to at least once per 12 hours. 
    This increase is consistent with standard industry practice as 
    represented by the Standard Technical Specifications (STS), Reference 
    1.
        2. Does the proposed license amendment create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated?
        A. Establishing operating personnel work hours at, ``an 8 to 12 
    hour day, nominal 40 hour week,'' allows normal plant operations to be 
    managed more effectively and does not adversely effect performance of 
    operating personnel. If 8 hour shifts are maintained in part or whole, 
    then acceptable levels of performance from operating personnel is 
    assured through effective control of shift turnovers and plant 
    activities. Overtime remains controlled by site administrative 
    procedures in accordance with the NRC Policy Statement on working hours 
    (Generic Letter 82-12). No physical modification of the plant is 
    involved. As such, the change does not introduce any new failure modes 
    or conditions that may create a new or different accident. Therefore, 
    operation in accordance with the proposed amendment will not create the 
    possibility of a new or different kind of accident from any previously 
    evaluated.
        B. Editorial changes clarify section 6.2.2.g without changing the 
    intent or meaning. The proposed change meets the intent of the NRC 
    Policy Statement on working hours (Generic Letter 82-12).
        C. Changes to sections 3.10.6.1.a and 3.10.9 do not change the 
    intent or meaning of the technical specification sections. 
    Clarification to the table notation in section 4.1 related to the 
    definition of shift checks to monitor plant conditions will continue as 
    intended but are allowed to increase up
    
    [[Page 59921]]
    
    to at least once per 12 hours. This increase is consistent with 
    standard industry practice as represented by the Standard Technical 
    Specifications (STS), Reference 1.
        3. Does the proposed amendment involve a significant reduction in a 
    margin of safety?
        A. Establishing operating personnel work hours at, ``an 8 to 12 
    hour day, nominal 40 hour week,'' allows normal plant operations to be 
    managed more effectively and does not adversely effect performance of 
    operating personnel. If 8 hour shifts are maintained in part or whole, 
    then acceptable levels of performance from operating personnel is 
    assured through effective control of shift turnovers and plant 
    activities. Overtime remains controlled by site administrative 
    procedures in accordance with the NRC Policy Statement on working hours 
    (Generic Letter 82-12) and is consistent with the Standard Technical 
    Specifications. The proposed change involves no physical modification 
    of the plant, or alterations to any accident or transient analysis. 
    There is no Basis to section 6 of the Technical Specifications, and the 
    changes are administrative in nature. Therefore, the change does not 
    involve any significant reduction in a margin of safety.
        B. Editorial changes clarify section 6.2.2.g without changing the 
    intent or meaning. The proposed change meets the intent of the NRC 
    Policy Statement on working hours (Generic Letter 82-12).
        C. Changes to sections 3.10.6.1.a and 3.10.9 do not change the 
    intent or meaning of the technical specification sections. 
    Clarification to the table notation in section 4.1 related to the 
    definition of shift checks to monitor plant conditions will continue as 
    intended but are allowed to increase up to at least once per 12 hours. 
    This increase is consistent with standard industry practice as 
    represented by the Standard Technical Specifications (STS), Reference 
    1.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, NY 10601.
        Attorney for licensee: Mr. David Blabey, 10 Columbus Circle, New 
    York, NY 10019.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. Ginna 
    Nuclear Power Plant, Wayne County, NY
    
        Date of amendment request: September 29, 1997, as supplemented 
    October 8, 1997. The September 29 application and October 8, 1997, 
    supplement supersede the September 13, 1996, application and its April 
    24, 1997, supplement. This notice supersedes the notice published on 
    October 9, 1996 (61 FR 197) in its entirety.
        Description of amendment request: The proposed amendment would 
    change the Ginna Station Technical Specifications (TSs) which would 
    allow referencing of revision of the Ginna Station pressure and 
    temperature limits report (PTLR) for the reactor coolant system (RCS) 
    pressure and temperature (P/T) limits and low temperature overpressure 
    protection (LTOP) limits. The proposed amendment would correct some 
    typographical errors in the TSs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes revise Administrative Controls Section 5.6.6.c 
    to update the reference to the NRC's approval of the first use of the 
    PTLR methodology, update the RCS P/T methodology to the final NRC 
    approved version, allow use of ASME Code Case N-514 for LTOP enable 
    temperature methodology, and to correct a typographical error. These 
    changes complete implementation of Generic Letter 96-03 by referencing 
    NRC approved methodology within the Administrative Controls. The 
    updated RCS P/T methodology has been generically approved by the NRC 
    while the use of ASME Code Case N-514 for LTOP enable temperature 
    methodology was previously approved for use at Ginna Station by the 
    NRC. As such, these changes are administrative in nature and do not 
    impact initiators or analyzed events or assumed mitigation of accident 
    or transient events. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an accident 
    previously analyzed.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The proposed changes 
    do not involve a physical alteration of the plant (i.e., no new or 
    different type of equipment will be installed) or changes in the 
    methods governing normal plant operation. The proposed changes will not 
    impose any new or different requirements. Thus, this change does not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of safety. 
    The proposed changes will not reduce a margin of plant safety because 
    the methodology have been shown to ensure that the P/T and LTOP limits 
    in the PTLR continue to meet all necessary requirements for reactor 
    vessel integrity. These changes are administrative in nature since the 
    limits were previously relocated to the PTLR under a separate LAR 
    [License Amendment Request]. As such, no question of safety is 
    involved, and the change does not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Rochester Public Library, 115 
    South Avenue, Rochester, NY 14610.
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, CA
    
        Date of amendment requests: December 22, 1995.
        Description of amendment requests: The licensee proposes to delete 
    the physical protection program reporting requirement from License 
    Condition 2.G, and to clarify in License Condition 2.E that all the 
    documents composing the physical protection program plans may not 
    contain safeguards information.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the
    
    [[Page 59922]]
    
    issue of no significant hazards consideration, which is presented 
    below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        This proposed change is considered an administrative change. It has 
    no impact on the probability or consequences of any of the accidents 
    previously evaluated. This change revises license conditions for 
    clarification and removes the burden of duplicate reporting 
    requirements. This change does not affect the physical protection 
    program as previously approved by the Nuclear Regulatory Commission 
    (NRC). License Condition 2.E is being revised to clarify that the 
    physical security, security force training and qualification, and 
    safeguards contingency plans may or may not contain safeguards 
    information. The security force training and qualification plan does 
    not currently contain safeguards information.
        A reporting requirement in License Condition 2.G is being revised 
    to remove the reference to License Condition 2.E for the physical 
    protection program. The reporting requirements for the physical 
    protection program are located in the regulations, 10 CFR 73.71 and 10 
    CFR 73 part, Appendix G.
        Therefore, the probability and consequences of an accident 
    previously evaluated are not affected by these proposed changes.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        This proposed change is considered an administrative change. It has 
    no impact on equipment, systems, or structures such that a new or 
    different kind of accident is created. This change revises license 
    conditions to clarify that safeguards information may be located in the 
    physical protection program plans and to remove duplicate and 
    unnecessary reporting requirements for the physical protection program. 
    There is no change associated with the implementation and maintenance 
    of the physical protection program as previously approved by the NRC.
        Therefore, the possibility of a new or different kind of accident 
    from an accident previously evaluated is not created.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        This proposed change is considered an administrative change only. 
    It has no impact on the margin of safety associated with the physical 
    protection program. This change revises license conditions to clarify 
    the location of safeguards information in the physical protection 
    program plans and remove duplicative and unnecessary reporting 
    requirements for the physical protection program. The maintenance and 
    implementation of the physical protection program is not affected by 
    this change.
        Therefore, there will not be a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, CA 92713.
        Attorney for licensee: T.E. Oubre, Esquire, Southern California 
    Edison Company, P.O. Box 800, Rosemead, CA 91770.
        NRC Project Director: William H. Bateman.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, OH
    
        Date of amendment request: October 22, 1997.
        Description of amendment request: The amendment would change the 
    Perry Nuclear Power Plant design basis as described in the Updated 
    Safety Analysis Report. The change will add a description of the 
    temperature control valves and associated bypass lines around the 
    Emergency Closed Cooling System heat exchangers. These features are 
    designed to ensure operability of the Control Complex Chilled Water 
    System under post-accident load conditions, without the need for 
    compensatory actions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed amendment is requesting Nuclear Regulatory Commission 
    (NRC) review and approval of changes to the Perry Nuclear Power Plant 
    (PNPP) Updated Safety Analysis Report (USAR) to incorporate 
    descriptions (in the form of text, tables and drawings) of a 
    modification to the plant involving two temperature control valves and 
    associated temperature elements, and piping segments that have been 
    installed in the Emergency Closed Cooling Water (ECC) System. These 
    valves, temperature elements, and piping segments were installed to 
    increase the overall reliability of the ECC System and the other safety 
    related plant systems that it serves, to help ensure that they perform 
    their specified safety functions without reliance on manual throttling 
    actions.
        The probability of occurrence and the consequences of an accident 
    previously evaluated in the USAR are not considered to be increased as 
    a result of the temperature control valve modification.
        Based on conformance with the original system design criteria, the 
    fact that the ECC System is an accident mitigation system, and that 
    this modification does not introduce any new initiators to a previously 
    postulated accident, the addition of this temperature control function 
    can not increase the probability of occurrence of an accident 
    previously evaluated in the USAR. Accidents reviewed involve the Loss 
    of Coolant Accident applications described in USAR Chapter 6 with their 
    corresponding consequence postulations shown in USAR Chapter 15, 
    accident and transient scenarios as described in USAR Chapter 15, 
    flooding and rupture postulations as described in USAR Chapter 3, and 
    fire protection analyses as described in USAR Chapter 9.
        The modification has been designed, procured, and installed to the 
    original design codes and standards. The modification also satisfies 
    single failure criteria and does not adversely affect the mitigation 
    function of the ECC System. Therefore, the ability to mitigate 
    accidents previously evaluated in the USAR is maintained and the 
    radiological consequences of such accidents remain unaffected.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of previously evaluated 
    accidents.
        2. The proposed change would not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The modification has been designed to satisfy the requirements of 
    the original ECC System. A single failure of the new configuration will 
    not result in more than the loss of one respective
    
    [[Page 59923]]
    
    ECC System loop as already analyzed. Analysis of flooding shows no 
    scenario greater than the currently bounding event. Missile generation 
    is not a concern since no mechanisms conducive to that potential have 
    been introduced. From the electrical analysis perspective, analysis has 
    shown no adverse effects on the Emergency Diesel Generator loadings or 
    other system applications.
        Based on the above discussions, the proposed change would not 
    create the possibility of a new or different kind of accident than 
    those previously evaluated.
        3. The proposed change will not involve a significant reduction in 
    the margin of safety.
        This request does not involve a significant reduction in a margin 
    of safety. The modification, including design, procurement, and 
    installation, has been performed in accordance with the applicable 
    codes, standards, and installation specifications. The modification 
    does not change the heat removal capabilities or any previously 
    designed parameters of the ECC System. Hence, the ECC System margin of 
    safety with respect to safety classification, protection, redundancy, 
    heat removal capability, and seismic classification remains unaffected.
        The margins of safety contained in the Technical Specifications and 
    the associated Bases also remain unaffected by this modification due to 
    conformance with the applicable codes, standards, and installation 
    specifications. Specifically, Technical Specification 3.7.10, 
    ``Emergency Closed Cooling Water (ECCW) System'' and the description in 
    the Bases remain unchanged and fully applicable. The following 
    Technical Specifications also remain unaffected and applicable: 
    3.3.3.2, ``Remote Shutdown System''; 3.7.1, ``Emergency Service Water 
    (ESW) System--Divisions 1 and 2''; 3.7.4, ``Control Room Heating, 
    Ventilation, and Air Conditioning (HVAC) System''; and the Technical 
    Specifications related to Sections 3.8 (Electrical Power Systems), 3.5 
    (Emergency Core Cooling Systems (ECCS) and Reactor Core Isolation 
    Cooling (RCIC) System) and 3.6 (Containment Systems). On this basis, 
    the margins of safety defined in the Technical Specifications remain 
    unchanged.
        Therefore, the changes associated with this license amendment 
    request do not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Gail H. Marcus.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, SC
    
        Date of application for amendment: August 27, 1996, as supplemented 
    December 18, 1996, January 17, February 18, March 27, April 4, April 
    25, April 29, May 30, June 2, June 13, June 18, August 4, August 8, 
    September 10, October 2 (RNP RA/97-0216), October 2, (RNP RA/97-0207), 
    October 13, and October 21, 1997.
        Brief description of amendment: This amendment addresses a more 
    restrictive change proposed by the licensee in minimum allowable 
    containment pressure.
        Date of publication of individual notice in Federal Register: 
    October 7, 1997 (62 FR 52362).
        Expiration date of individual notice: October 21, 1997.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, SC 29550.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, NJ
    
        Date of amendment request: September 24, 1997.
        Brief description of amendment request: The proposed amendment 
    would add a surveillance requirement in Section 3/4.5.1 to perform a 
    monthly valve position verification for each of the four residual heat 
    removal crosstie valves.
        Date of publication of individual notice in Federal Register: 
    October 6, 1997 (62 FR 52162).
        Expiration date of individual notice: November 5, 1997.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, NJ
    
        Date of amendment request: September 29, 1997.
        Brief description of amendment request: The proposed amendment 
    would change Technical Specification 3/4.11.1, ``Liquid Effluents--
    Concentration.'' The proposed change adds a requirement to perform 
    weekly sampling and monthly and quarterly composite analyses of the 
    Station Service Water System when the Reactor Auxiliaries Cooling 
    System is contaminated.
        Date of publication of individual notice in Federal Register: 
    October 6, 1997 (62 FR 52161).
        Expiration date of individual notice: November 5, 1997.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in
    
    [[Page 59924]]
    
    connection with these actions was published in the Federal Register as 
    indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 & 50-324, 
    Brunswick Steam Electric Plant, Units 1 & 2, Brunswick County, NC
    
        Date of amendment request: January 7, 1997, as supplemented on July 
    25, 1997, August 27, 1997, and September 15, 1997.
        Brief description of amendment: The amendments correct an error 
    involving the transposition of two of the reactor pressure vessel (RPV) 
    pressure-temperature (P-T) limits curves between the Technical 
    Specifications for the Brunswick Steam Electric Plant, Units 1 and 2 
    and update the hydrostatic pressure test limits curves for both units.
        Date of issuance: October 7, 1997.
        Effective date: October 7, 1997.
        Amendment No.: 189 and 220.
        Facility Operating License Nos. DPR-71 and DPR-62: Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: March 12, 1997 (62 FR 
    11485). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 7, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, NC 28403-3297.
    
    Carolina Power & Light Company, Docket No. 50-261, H.B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, SC
    
        Date of application for amendment: August 27, 1996, as supplemented 
    December 18, 1996, January 17, February 18, March 27, April 4, April 
    25, April 29, May 30, June 2, June 13, June 18, August 4, August 8, 
    September 10, October 2 (RNP RA/97-0216), October 2, (RNP RA/97-0207), 
    October 13, and October 21, 1997.
        Brief description of amendment: This amendment addresses a more 
    restrictive change proposed by the licensee in minimum allowable 
    containment pressure.
        Date of issuance: October 24, 1997.
        Effective date: October 24, 1997.
        Amendment No.: 176.
        Facility Operating License No. DPR-23: Amendment revises the 
    License and Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration (NSHC): Yes (62 FR 52362 dated October 7, 1997). The 
    notice provided an opportunity to submit comments on the Commission's 
    proposed NSHC determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by November 6, 
    1997, but indicated that if the Commission makes a final NSHC 
    determination, any such hearing would take place after issuance of the 
    amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final determination of NSHC are contained in 
    a Safety Evaluation dated October 24, 1997.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, SC 29550.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, NC
    
        Date of application for amendment: February 21, 1997.
        Brief description of amendment: This amendment adds a specific time 
    limit to Technical Specification Table 3.3-3 to place an inoperable 
    refueling water storage tank level channel in a bypassed condition.
        Date of issuance: September 30, 1997.
        Effective date: September 30, 1997.
        Amendment No: 74.
        Facility Operating License No. NPF-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 9, 1997 (62 FR 
    17225). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 30, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, NC 27605.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, IL
    
        Date of application for amendments: March 5, 1997 as supplemented 
    October 3, 1997.
        Brief description of amendments: The amendments would revise the 
    Technical Specifications by removing the main steamline radiation 
    monitor reactor scram function and the main steamline tunnel radiation 
    isolation function.
        Date of issuance: October 24, 1997.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 163, 158.
        Facility Operating License Nos. DPR-19 and DPR-25: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 18, 1997 (62 FR 
    19141). The October 3, 1997, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    October 24, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, IL 60450.
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, LA
    
        Date of amendment request: August 29, 1996, supplemented August 29, 
    1996 (proprietary), September 5, and October 8, 1997.
        Brief description of amendment: The amendment eliminates the 
    Average Power Range Monitor (APRM) setpoint T-Factor setdown 
    requirements and provides for reactivity anomaly calculation 
    improvements. The request to decrease the local power range
    
    [[Page 59925]]
    
    monitor (LPRM) calibration frequency will be handled by separate review 
    and action.
        Date of issuance: October 10, 1997.
        Effective date: October 10, 1997.
        Amendment No.: 100.
        Facility Operating License No. NPF-47: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1997 (61 FR 
    55032). The Licensee's letters dated August 29, 1996 (proprietary), 
    September 5, and October 8, 1997, provided additional clarification and 
    corrections to other TSs that would have erroneously referenced the TSs 
    being eliminated and did not change the staff's initial no significant 
    hazards determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, PA
    
        Date of application for amendment: July 30, 1997, as supplemented 
    September 19, and September 24, 1997.
        Brief description of amendment: The amendment reduces current 
    technical specification leakage limit from the decay heat removal 
    system from 6.0 gallons per hour (gph) to 0.6 gph.
        Date of issuance: October 15, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 205.
        Facility Operating License No. DPR-50: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 27, 1997 (62 FR 
    45458). The September 19, and September 24, 1997, submittals did not 
    affect the initial no significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 15, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, PA
    
        Date of application for amendment: August 12, 1997, as supplemented 
    August 28, September 15, October 3, 9, and 10, 1997.
        Brief description of amendment: The amendment changes the technical 
    specifications surveillance requirements for once-through steam 
    generator inservice inspection for Cycle 12 operation.
        Date of issuance: October 16, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 206.
        Facility Operating License No. DPR-50: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 27, 1997 (62 FR 
    45458). The supplemental letters did not affect the initial no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 16, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, TX, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, TX
    
        Date of amendment request: August 14, 1997, as supplemented 
    September 23, 1997. The supplement provided clarifying information 
    within the scope of the amendment request and did not change the 
    initial no significant hazards consideration determination.
        Brief description of amendments: The amendments revise the allowed 
    tolerance of the reactor coolant system volume provided in Technical 
    Specification 5.4.2 to account for steam generator tube plugging.
        Date of issuance: October 20, 1997.
        Effective date: October 20, 1997.
        Amendment Nos.: Unit 1--Amendment No. 92; Unit 2--Amendment No. 79.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 26, 1997 (62 FR 
    45278). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 20, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J.M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone Nuclear 
    Power Station, Unit 1, New London County, CT
    
        Date of application for amendment: February 7, 1997, as 
    supplemented April 3 and September 19, 1997.
        Brief description of amendment: The amendment clarifies the 
    requirement for calibration of instrument channels that use resistance 
    temperature detectors or thermocouples.
        Date of issuance: October 22, 1997.
        Effective date: As of the date of issuance, to be implemented 
    within 90 days.
        Amendment No.: 102.
        Facility Operating License No. DPR-21: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 9, 1997 (62 FR 
    17236). The April 3 and September 19, 1997, letters provided additional 
    and clarifying information that did not change the scope of the 
    February 7, 1997, application and the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 22, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT, and at the Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, CT
    
        Date of application for amendment: June 19, 1997.
        Brief description of amendment: Technical Specification Table 2.2-1 
    NOTES 1 and 3 define the values for the constants used in the 
    Overtemperature Delta-T and Overpower Delta-T reactor trip system 
    instrumentation setpoint calculators. The amendment makes changes to 
    the NOTES as well as the associated Bases section.
    
    [[Page 59926]]
    
        Date of issuance: October 22, 1997.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 152.
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 30, 1997 (62 FR 
    40852). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 22, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT, and the Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County, MI
    
        Date of application for amendments: November 6, 1996, as 
    supplemented April 10 and October 1, 1997.
        Brief description of amendments: The amendments revise Technical 
    Specifications governing the cooling water system and are a partial 
    response to the licensee's application. The changes improve plant 
    operation based on operational experience with the vertical motor-
    driven cooling water pump. The changes also incorporate information 
    gathered by the licensee during its self-assessment Service Water 
    System Operational Performance Inspection (SWSOPI) completed in late 
    1995. The remainder of the licensee's application will be addressed in 
    a separate licensing action.
        Date of issuance: October 21, 1997.
        Effective date: October 21, 1997, with full implementation within 
    90 days.
        Amendment Nos.: 131 and 123.
        Facility Operating License Nos. DPR-42 and DPR-60: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4338) The April 10 and October 1, 1997, letters provided clarifying 
    information within the scope of the original application and did not 
    change the staff's initial proposed no significant hazards 
    considerations determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 21, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, MI 
    55401.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket No. 
    50-278, Peach Bottom Atomic Power Station, Unit No. 3, York County, PA
    
        Date of application for amendment: June 30, 1997, as supplemented 
    by letter dated September 26, 1997.
        Brief description of amendment: Revises the minimum critical power 
    ratio (MCPR) safety limit in Section 2.1 of the Technical 
    Specifications from 1.07 to 1.11 for two recirculation loops in 
    operation. For a single loop in operation, the MCPR will change from 
    1.08 to 1.12. The new MCPR safety limits reflect the effect of the new 
    General Electric--13 part length fuel design and other Peach Bottom 
    core-specific parameters.
        Date of issuance: October 9, 1997.
        Effective date: As of the date of issuance, to be implemented prior 
    to startup from Unit 3 refueling outage 3R11.
        Amendment No.: 225.
        Facility Operating License No. DPR-56: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 13, 1997 (62 FR 
    43373).
        The supplemental letter provided clarifying information that did 
    not change the original no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 9, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, PA
    
        Date of application for amendments: April 9, 1997.
        Brief description of amendments: These amendments revise the TSs to 
    clarify existing battery-specific gravity requirements, delete the 
    requirement to correct specific gravity values based on electrolyte 
    level, and allow the use of charging current measurements to verify the 
    battery's state of charge.
        Date of issuance: October 8, 1997.
        Effective date: Both units, as of date of issuance and shall be 
    implemented within 30 days.
        Amendment Nos.: 123 and 88.
        Facility Operating License Nos. NPF-39 and NPF-85: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 4, 1997 (62 FR 
    30643).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 8, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
    364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, AL
    
        Date of amendments request: March 7, 1997.
        Brief Description of amendments: The amendments change the 
    Technical Specifications for both Farley units to allow operability 
    testing for certain containment isolation valves during defueled 
    status.
        Date of issuance: October 17, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1--130; Unit 2--123.
        Facility Operating License Nos. NPF-2 and NPF-8: Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19834).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 17, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, AL 36302.
    
    Southern Nuclear Operating Company, Inc., Docket No. 50-348, Joseph M. 
    Farley Nuclear Plant, Unit 1, Houston County, AL
    
        Date of amendment request: September 3, 1997.
        Brief Description of amendment: The changes reduce the number of 
    required incore detectors necessary for continued operation for the 
    remainder of Cycle 15 only.
        Date of issuance: October 23, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 131.
    
    [[Page 59927]]
    
        Facility Operating License No. NPF-2: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 10, 1997 (62 
    FR 47695).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 23, 1997.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, AL.
    
    Tennessee Valley Authority, Docket No. 50-390 Watts Bar Nuclear Plant, 
    Unit 1, Rhea County, TN
    
        Date of application for amendment: June 20, 1997.
        Brief description of amendment: Modify the Watts Bar Technical 
    Specifications (TS) to incorporate the use of Code Case N-514 into the 
    methodology for the Pressure-Temperature Limits Report.
        Date of issuance: October 21, 1997.
        Effective date: October 21, 1997.
        Amendment No.: 9.
        Facility Operating License No. NPF-90: Amendment revises the TS.
        Date of initial notice in Federal Register: September 10, 1997 (62 
    FR 47700).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 21, 1997.
        No significant hazards consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, KS
    
        Date of amendment request: July 3, 1997, as supplemented by letter 
    dated August 20, 1997.
        Brief description of amendment: The amendment revises Surveillance 
    Requirements 4.3.1.2 and 4.3.2.2, and Technical Specifications 3/4.3.1 
    and 3/4.3.2, and associated Bases Sections B 3/4.3.1 and B 3/4.3.2 to 
    eliminate periodic response time testing requirements for selected 
    pressure and differential pressure sensors in the reactor trip system 
    and engineered safety features actuation system instrumentation 
    channels.
        Date of issuance: October 20, 1997.
        Effective date: October 20, 1997, to be implemented prior to 
    restart from the ninth refueling outage currently scheduled to start on 
    October 4, 1997.
        Amendment No.: 113.
        Facility Operating License No. NPF-42: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 30, 1997 (62 FR 
    40862).
        The August 20, 1997, supplemental letter provided additional 
    clarifying information and did not change the initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    October 20, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, KS 66801 
    and Washburn University School of Law Library, Topeka, KS 66621.
    
        Dated at Rockville, Maryland, this 29th day of October 1997.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 97-29138 Filed 11-4-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
10/7/1997
Published:
11/05/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-29138
Dates:
October 7, 1997.
Pages:
59912-59927 (16 pages)
PDF File:
97-29138.pdf