94-27613. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 216 (Wednesday, November 9, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 94-27613]
    
    
    [[Page Unknown]]
    
    [Federal Register: November 9, 1994]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
     
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from October 17, 1994, through October 28, 1994. 
    The last biweekly notice was published on October 26, 1994 (59 FR 
    53834).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By December 9, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-800-
    248-5100 (in Missouri 1-800-342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Carolina Power & Light Company, et al.
    
    Docket Nos. 50-325 and 50-324
    
        Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, 
    North Carolina.
        Date of amendments request: September 30, 1994.
        Description of amendments request: The amendments would revise the 
    Technical Specifications to eliminate the scram and isolation trip 
    functions from the main steam line radiation monitor (MSLRM). This 
    change would specifically remove the reactor scram, main steam line 
    isolation valve closure, main steam line drain valve closure, reactor 
    water sample line isolation, and mechanical vacuum pump line isolation 
    actuated on a MSLRM High-High Radiation signal. The actuation signal 
    for isolation of the reactor water sample line will be replaced with a 
    low condenser vacuum signal. The isolation of the mechanical vacuum 
    pump line will be changed to a signal from the main stack radiation 
    monitor.
        The MSLRMs will have both High Radiation and High-High Radiation 
    alarms. The setpoint for the MSLRM High Radiation alarm will be set at 
    or below 1.5 times the nominal full power background radiation adjusted 
    for Hydrogen water chemistry operation. The setpoint for the condenser 
    off-gas radiation monitor will be set at a value of 1.5 times 
    background radiation, but not less than 1.5 Rem per hour.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The deletion of the MSLRM trip function from the reactor scram and the 
    Group 1 isolation initiation logic removes a potential transient 
    initiation and therefore decreases the probability of plant transients 
    occurring due to inadvertent scrams resulting from this system.
        The deletion of the MSLRM trip function from the Main Steam Drain 
    Valve, the Reactor Water Sample Isolation Valve, and the Mechanical 
    Vacuum Pump line isolation logic, does not affect the initiators of any 
    accident previously evaluated in the Safety Analysis Report. Therefore, 
    the proposed change does not involve an increase in the probability of 
    occurrence of any accident previously evaluated.
        The NRC staff acceptance criterion for the Control Rod Drop 
    Accident is that the doses from the accident fall significantly below 
    the limits given in 10 CFR Part 100. The releases calculated for 
    accident during plant operations when the Steam Jet Air Ejectors (SJAE) 
    are operating and when the Mechanical Vacuum Pumps are operating are 
    within these acceptance limits.
        In NEDO-31400, GE shows that the occurrence of a CRDA, with the MSL 
    high radiation isolation removed, and SJAE in operation, results in 
    offsite radiological exposures that are small fractions of 10CFR100 
    guidelines. Since the Brunswick specific CRDA doses are lower than the 
    [sic] calculated by GE and the GE dose parameters envelope those used 
    for the Brunswick analysis, it is concluded that the NRC's findings 
    that the radiological release consequence is within the staff's 
    acceptance criteria, even without the automatic MSIV trip, is 
    applicable to Brunswick.
        While not specifically addressed in the GE evaluation, Carolina 
    Power and Light also proposes to eliminate the Main Steam Line Drain 
    valves, the Reactor Water Sample Line isolation valves, and the 
    mechanical vacuum line isolation valves from the MSLRM isolation logic. 
    Main Steam Line Drain Valves B21-F016 and B21-F019 drain to the main 
    condenser, which is the same flow path as the MSIVs. The discharge of 
    both the MSIV and MSL drain flow paths is processed through the offgas 
    system. Any radiation released through the drain valves during a 
    control rod drop accident will be negligible and, for Brunswick, is 
    bounded by the NEDO analysis.
        The reactor water sample line provides a small amount of reactor 
    water to the Reactor Building Sample Panel. The discharge of the 
    Reactor Building Sample Panel is routed through the floor drain sump to 
    the liquid radwaste system. Any releases through this path would be 
    negligible and, for Brunswick, is bounded by the NEDO analysis.
        The mechanical vacuum pumps are used only when the reactor is at 
    low power (less than 5%) and there is insufficient steam flow to 
    operate the Steam Jet Air Ejectors. The increase in radiation will be 
    detected by the MSLRMs and annunciated in the Main Control Room. 
    Operators will be instructed, in the annunciator response procedures, 
    to take action to stop the Mechanical Vacuum Pump(s) and isolate the 
    Mechanical Vacuum Pump line. The amount of radiation released prior to 
    isolating the line would represent the most limiting case for this 
    accident. However, it will still be well within 10 CFR Part 100 limits. 
    Additionally, the dose received in the Main Control Room as a result of 
    this accident is within General Design Criteria 19 (SRP 6.4) limits.
        Therefore, since elimination of the MSIV [sic, MSLRM] scram and 
    isolation functions would not result in an increase in exposure above 
    NRC acceptance limits, the proposed changes will not significantly 
    increase the consequences of a previously evaluated accident.
        2. The proposed amendments would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The function of a MSLRM trip is to detect abnormal fission 
    product release and isolate the steam lines, thereby stopping the 
    transport of fission products from the reactor to the main condenser. 
    The monitors do not perform a prevention function for any kind of 
    accident. The existence of a MSLRM trip does not prevent the occurrence 
    of a fuel failure event or any other type of event. The elimination of 
    these signals, which served only in a mitigative function, does not 
    create the possibility of a new or different kind of accident from 
    those previously evaluated. Also, radiation monitors with alarm 
    functions will remain installed in the plant to warn the operators of a 
    high radiation condition in the main steam lines, or in the off-gas 
    system. Thus no new or different accident can be postulated by the 
    proposed changes.
        3. The proposed amendments do not involve a significant reduction 
    in a margin of safety. As shown in the topical report, the changes 
    represent an overall improvement in plant safety. Safe operation of the 
    plant is further enhanced by elimination of the unnecessary scram and 
    isolation of the reactor vessel. With implementation of these changes, 
    1) the primary heat sink (main condenser) remains available, 2) large 
    transients on the reactor vessel, as well as challenges to the ESF, are 
    avoided, and 3) the Offgas system remains available to control the 
    pathway of potential releases. As such, the margin of safety is 
    enhanced by the proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
        NRC Acting Project Director: Michael L. Boyle.
    
    Carolina Power & Light Company
    
    Docket No. 50-261
    
        H. B. Robinson Steam Electric Plant, Unit No. 2, Darlington County, 
    South Carolina.
        Date of amendment request: October 7, 1994.
        Description of amendment request: The proposed amendment would 
    revise the introduction to TS Section 6.9.3.3 to require the approved 
    revision number for the referenced analytical methods be listed in the 
    Core Operating Limits Report. The methodology referenced in 6.9.3.3.b.f 
    (XN-NF-82-49(A)) will be updated to clarify that all supplements are 
    included. New methodologies ANF-89-151(A) and EMF-92-081(A) will be 
    added to TS Section 6.9.3.3.b.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated. 
    The proposed changes will have no influence on the probability of an 
    accident previously evaluated. No changes will be made to any safety 
    related equipment, systems, or setpoints used in determining the 
    probability of an evaluated accident. The plant design basis will not 
    be altered. Therefore, there will be no significant increase in the 
    probability of an accident previously evaluated.
        Consequences are dependent on the type of accident and the 
    mitigating response of safety related equipment. Furthermore, the 
    magnitude of consequences are calculated, directly or through 
    supporting calculations, by use of NRC approved methodologies. The 
    proposed license amendment will not alter the function of safety 
    related equipment designed to mitigate the consequences of an accident 
    previously evaluated or allow operation of the facility outside any 
    current limitations or restrictions. Also, this amendment will not 
    alter the requirement that evaluation of the consequences of an 
    accident previously evaluated by determined/supported with NRC reviewed 
    and approved methodologies. The change to TS Section 6.9.3.3.b's 
    introductory wording satisfies an administrative commitment and the 
    requirements it adds are administrative in nature. Accordingly the 
    proposed license amendment will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated. 
    The addition of and update to NRC previously reviewed and approved 
    methodologies in TS Section 6.9.3.3.b will not result in any design or 
    function changes to any safety related equipment designed to prevent 
    and/or mitigate accidents, to any setpoints or systems, or to any 
    portion of the plant design basis. Operation of the facility will 
    remain within all required limitations and/or restrictions. The change 
    to TS Section 6.9.3.3.b's introductory wording satisfies an 
    administrative commitment and the requirements it adds are 
    administrative in nature. Therefore, the proposed amendment will not 
    create the possibility of a new kind of accident from any accident 
    previously evaluated.
        The addition of and update to NRC previously reviewed and approved 
    methodologies in TS Section 6.9.3.3.b will not result in any design or 
    function changes to any safety related equipment designed to prevent 
    and or mitigate accidents, to any setpoints or systems, or to any 
    portion of the plant design basis. Operation of the facility will 
    remain within all required limitations and/or restrictions. The changes 
    to TS Section 6.9.3.3.b's introductory wording satisfies an 
    administrative commitment and the requirements it adds are 
    administrative in nature. Therefore, the proposed amendment will not 
    create the possibility of a different kind of accident from any 
    accident previously evaluated.
        3. The proposed amendment does not involve a significant reduction 
    in the margin of safety. The proposed license amendment is defined as 
    administrative in nature. No current operational limits, restrictions, 
    or operating modes of the facility and its equipment, safety related or 
    otherwise, designed to preserve the margin of safety will be changed or 
    affected by the proposed amendment. There will be no changes to 
    setpoints or to the plant design basis. The methodology proposed for 
    addition to TS Section 6.9.3.3.b and the methodology that will be 
    updated has been previously reviewed and approved by the NRC. The 
    change to TS Section 6.9.3.3.b's introductory wording satisfies an 
    administrative commitment and the requirements it adds are 
    administrative in nature. Accordingly the proposed license amendment 
    will not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: R.E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
        NRC Project Director: William H. Bateman.
    
    Entergy Operations, Inc., et al.
    
    Docket No. 50-416
    
        Grand Gulf Nuclear Station, Unit 1, Claiborne County, Mississippi.
        Date of amendment request: October 12, 1994.
        Description of amendment request: The proposed amendment requests 
    the closure and deletion of License Condition 2.C.(26) related to 
    turbine disk integrity.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. No significant increase in the probability or consequences of an 
    accident previously evaluated results from this change.
        The proposed change would close and delete License Condition 
    2.C.(26). The approved methodology currently used to evaluate the 
    probability of rotor failure and the inspection interval will not be 
    changed. The closure and deletion of the license condition is an 
    administrative change and will affect any accident previously 
    evaluated.
        The bounding accident for the turbine-generator as analyzed in the 
    Grand Gulf Nuclear Station (GGNS) Updated Final Safety Analysis Report 
    (UFSAR) is the occurrence of an external missile resulting from the 
    failure of a low pressure (LP) turbine disc. The probability of this 
    incident occurring is less than 1 x 10-5 per year, which is the 
    NRC acceptable failure criterion for probability.
        Any extension to the service interval in the future will be 
    evaluated in accordance with the current methodology. The original 
    acceptable levels of failure will be maintained. Therefore, no 
    significant increase in the probability or consequences of a previously 
    evaluated accident results from this change.
        2. The change would not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The proposed change does not involve a change to the control logic 
    or operating procedures for the turbine but rather transfers the 
    control of the LP turbine disc inspection interval from the Operating 
    License to administrative control. The current approved methodology 
    will continue to be used when determining future inspection intervals.
        Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The change would not involve a significant reduction in a margin 
    of safety.
        Closing and deleting the current license condition for LP turbine 
    disc inspections and controlling the inspection interval 
    administratively has no adverse effects to the margin of safety. The 
    current approved methodology for failures will continue to be used and 
    any changes to future inspection intervals will be evaluated by the 
    methodology. This change does not affect any previous safety analysis 
    presented in the UFSAR and does not affect the criteria used to 
    establish safety limits, the basis for limiting safety system settings, 
    the basis for limiting conditions of operation, a change to the 
    technical specifications or a change in plant operations.
        Therefore, this change does not involve a significant reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, Mississippi 39120.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Florida Power and Light Company
    
    Docket Nos. 50-250 and 50-251
    
        Turkey Point Plant, Units 3 and 4, Dade County, Florida.
        Date of amendment request: October 20, 1994.
        Description of amendment request: The licensee proposes to change 
    Turkey Point, Units 3 and 4 Technical Specifications (TS) by revising 
    TS 1.9, Definitions--CORE ALTERATIONS to only address activities which 
    may, in actuality, affect core reactivity. In addition, the licensee 
    proposes to revise TS 3.9.4, Containment Building Penetrations to allow 
    both containment personnel airlock (PAL) doors to be open during core 
    alterations and movement of irradiated fuel in containment provided (a) 
    that at least one PAL door is capable of being closed; (b) the plant is 
    in Mode 6 with at least 23 feet of water above the fuel; and (c) a 
    designated individual is available outside the PAL to close the door. 
    The licensee also proposes a revision to the footnote of TS 3.9.4, to 
    remove the description of the purpose for imposing administrative 
    controls.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The change in the definition of CORE ALTERATIONS would allow the 
    movement of a temporary source range detector or other small 
    components, such as cameras, tools, etc., within the reactor vessel 
    without the activity being considered CORE ALTERATIONS. The potential 
    exists, however small, that an object can be dropped into the reactor 
    vessel. However, the justification for this change, is that the 
    insertion of small components into the reactor vessel will have no 
    effect on core reactivity since these items displace a small volume of 
    borated water, and sufficient borated water will surround the 
    components and provide the necessary neutron absorption to 
    neutronically isolate the components from the reactor. The consequences 
    of dropping one of these small components into the vessel are bounded 
    by the In-Containment Fuel Handling Accident Analysis discussed in 
    Chapter 14.2.1 of the Turkey Point Updated Final Safety Analysis Report 
    (UFSAR). Therefore, the proposed change is bounded by the current and 
    the proposed In-Containment Fuel Handling Accident Analyses and will 
    not involve a significant increase in the probability or consequences 
    of an accident previously evaluated.
        The proposed change to TS 3.9.4 would allow the containment 
    personnel airlock (PAL) doors to be open during fuel movement and core 
    alterations. Currently, a single PAL door is closed during fuel 
    movement and core alterations to prevent the escape of radioactive 
    material in the event of a in-containment fuel handling accident. The 
    PAL is not an initiator of an accident. Whether the PAL doors are open 
    or closed during fuel movement and core alterations has no affect on 
    the probability of any accident previously evaluated.
        Allowing the PAL doors to be open during fuel movement and core 
    alterations does not increase the consequences from a fuel handling 
    accident. The calculated offsite doses are well within the limits of 10 
    CFR Part 100. In addition, the calculated doses are larger than the 
    expected doses because the calculation does not incorporate the closing 
    of the PAL door after the containment is evacuated. The proposed change 
    should significantly reduce the dose to workers in containment in the 
    event of a fuel handling accident by reducing the time required to 
    evacuate the containment. The proposed change will also significantly 
    decrease the wear on the PAL doors and, consequently, increase the 
    availability of the PAL doors in the event of an accident.
        The proposed change to the footnote of TS 3.9.4 is administrative 
    in nature, and does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The changes being proposed do not affect assumptions contained in 
    plant safety analyses or the physical design of the plant, nor do they 
    affect Technical Specifications that preserve safety analysis 
    assumptions. Therefore, operation of the facility in accordance with 
    the proposed amendments would not involve a significant increase in the 
    probability or consequences of an accident previously analyzed.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The change in the definition of CORE ALTERATIONS would allow the 
    movement of a temporary source range detector or other small 
    components, such as cameras, tools, etc., within the reactor vessel 
    without the activity being considered CORE ALTERATIONS. The potential 
    exists however small, that an object can be dropped into the reactor 
    vessel. However, the justification for this change, is that the 
    insertion of small components into the reactor vessel will have no 
    effect on core reactivity since these items displace a small volume of 
    borated water, and sufficient borated water will surround the 
    components and provide the necessary neutron absorption to 
    neutronically isolate the components from the reactor. The consequences 
    of dropping one of these small components into the vessel are bounded 
    by the In-Containment Fuel Handling Accident Analysis discussed in 
    Chapter 14.2.1 of the Turkey Point UFSAR. Therefore the proposed change 
    is bounded by the current and the proposed In-Containment Fuel Handling 
    Accident Analyses and will not create the possibility of a new or 
    different kind of accident.
        The proposed change to Specification 3.9.4 affects a previously 
    evaluated accident, i.e., in-containment fuel handling accident. Both 
    the current and the proposed In-Containment Fuel Handling Accident 
    Analysis assume that all of the iodines and noble gases that become 
    airborne within the containment escape and reach the site boundary and 
    low population zone with no credit taken for the containment building 
    barrier or for decay or deposition taken. Since the proposed change 
    does not involve the addition or modification of equipment nor does it 
    alter the design of plant systems and the revised analysis is 
    consistent with the current In-Containment Fuel Handling Accident 
    Analysis, the proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed change to the footnote of TS 3.9.4 is administrative 
    in nature and does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The change in the definition of CORE ALTERATIONS would allow the 
    movement of a temporary source range detector or other small 
    components, such as cameras, tools, etc., within the reactor vessel 
    without the activity being considered CORE ALTERATIONS. The potential 
    exists however small, that an object can be dropped into the reactor 
    vessel. However, the justification for this change, is that the 
    insertion of small components into the reactor vessel will have no 
    effect on core reactivity since these items displace a small volume of 
    borated water, and sufficient borated water will surround the 
    components and provide the necessary neutron absorption to 
    neutronically isolate the components from the reactor. The consequences 
    of dropping one of these small components into the vessel are bounded 
    by the Fuel Handling Accident Analysis discussed in Chapter 14.2.1 of 
    the Turkey Point UFSAR. Therefore, the proposed change is bound by the 
    current In-Containment Fuel Handling Accident Analyses and as a result 
    will not involve a significant reduction in a margin of safety.
        The margin of safety as defined by 10 CFR Part 100 has not been 
    reduced. There is no increase in calculated offsite dose resulting from 
    a fuel handling accident in containment and the calculated dose is a 
    small fraction of the limits given in 10 CFR Part 100. The proposed 
    changes do not alter the bases for assurance that safety-related 
    activities are performed correctly or the basis for any Technical 
    Specification that is related to the establishment of or maintenance of 
    a safety margin. Therefore, operation of the facility in accordance 
    with the proposed amendments would not involve a significant reduction 
    in a margin of safety.
        The proposed change to the footnote of TS 3.9.4 is administrative 
    in nature and does not relate to or modify the safety margins defined 
    in, and maintained by, the Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
        Attorney for licensee: Harold F. Reis, Esquire, Newman and Holtzer, 
    P.C., 1615 L Street, NW., Washington, DC 20036.
        NRC Project Director: Mohan C. Thadani, (Acting)
    
    Florida Power and Light Company
    
    Docket Nos. 50-250 and 50-251
    
        Turkey Point Plant, Units 3 and 4, Dade County, Florida.
        Date of amendment request: October 20, 1994.
        Description of amendment request: This supersedes the licensee's 
    original request dated July 19, 1994, and noticed in the Federal 
    Register on August 3, 1994 (59 FR 39588). The licensee proposes to 
    change Turkey Point, Units 3 and 4 Technical Specifications (TS) 
    4.8.1.1.2e. and 4.8.1.1.2f., which address Emergency Diesel Generator 
    (EDG) fuel oil testing, by replacing the specific EDG fuel oil 
    Surveillance Requirements with the requirement to verify new and stored 
    EDG fuel oil in accordance with the Diesel Fuel Oil Testing Program. In 
    addition, the licensee proposes the addition of ACTION statements g. 
    and h., to TS 3.8.1.1, to address the required action in the event the 
    diesel fuel oil does not meet the Diesel Fuel Oil Testing Program 
    limits. The Diesel Fuel Oil Testing Program will be described in both 
    TS 6.8.4 and the BASES Section to the Technical Specifications. In 
    addition, FPL proposes revising TS 6.8.1 to include the requirement 
    that written procedures shall be established, implemented and 
    maintained for implementation of the Diesel Fuel Oil Testing Program.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed changes to the Technical Specifications will permit 
    the Technical Specification required testing of Emergency Diesel 
    Generator (EDG) fuel oil in accordance with the Turkey Point, Units 3 
    and 4 Diesel Fuel Oil Testing Program. The proposed change will permit 
    FPL to use more recent editions of the American Society for Testing and 
    Materials (ASTM) standards currently listed in Technical Specification 
    Surveillance Requirements 4.8.1.1.2e. and 4.8.1.1.2f. Prior to changing 
    the Diesel Fuel Oil Testing Program, the proposed change will be 
    evaluated pursuant to Title 10 Code of Federal Regulations Sec. 50.59 
    (10 CFR Sec. 50.59), ``Changes, tests, and experiments.'' Title 10 CFR 
    Sec. 50.59 permits a licensee to make changes in the procedures as 
    described in the safety analysis report without prior Commission 
    approval, provided that the proposed changes does not involve an 
    unreviewed safety question.
        Title 10 CFR Sec. 50.59(a)(2) states that a proposed change 
    involves an unreviewed safety question (i) if the probability of 
    occurrence or the consequences of an accident or malfunction of 
    equipment important to safety previously evaluated in the safety 
    analysis report may be increased. Consequently, since any change to the 
    Diesel Fuel Oil Testing Program, including the ASTM standard or ASTM 
    edition standard to be used to evaluate EDG fuel oil acceptability, the 
    change must be evaluated relative to the more restrictive evaluation 
    criterion of 10 CFR Sec. 50.59, then operation of the facility in 
    accordance with the proposed amendments would not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated. The EDG fuel oil TS Surveillance Requirements will be 
    replaced with a requirement to test the EDG fuel oil in accordance with 
    the Turkey Point Units 3 and 4 Diesel Fuel Oil Testing Program.
        ACTION statement g. of TS 3.8.1.1 is added to address the required 
    action in the event the new fuel oil properties do not meet the Diesel 
    Fuel Oil Testing Program limits. A failure to meet the American 
    Petroleum Institute (API) gravity, kinematic viscosity, flash point or 
    clarity limits is cause for rejecting the new fuel oil prior to the 
    addition to the Diesel Fuel Oil Storage Tanks, but does not represent a 
    failure to meet the Limiting Condition for Operation (LCO) of TS 
    3.8.1.1, since the new fuel oil has not been added to the storage 
    tanks. Provided these new fuel oil properties are met subsequent to the 
    addition of the new fuel oil to the storage tanks, 30 days is provided 
    to complete the analyses of the other fuel oil properties specified in 
    Table 1 of ASTM-D975-81, except sulfur which may be performed in 
    accordance with ASTM-D1552-79 or ASTM-D2622-82. In the event the other 
    new fuel oil properties specified in Table 1 of ASTM-D975-81 are not 
    met, ACTION statement g. of TS 3.8.1.1 provides an additional 30 days 
    to meet the Diesel Fuel Oil Testing Program limits. This additional 30 
    day period is acceptable because the fuel oil properties of interest, 
    even if they are not within limits, would not have an immediate effect 
    on EDG operation.
        ACTION statement h. of TS 3.8.1.1 is added to address the required 
    action in the event the stored fuel oil total particulates do not meet 
    the Diesel Fuel Oil Testing Program limits. Fuel oil degradation during 
    long term storage shows up as an increase in particulate, due mostly to 
    oxidation. The presence of particulate does not mean the fuel oil will 
    not burn properly in a diesel engine. The frequency for performing 
    surveillance on stored fuel oil is based on stored fuel oil degradation 
    trends which indicate that particulate concentration is unlikely to 
    change significantly between surveillances.
        Prior to changing the Turkey Point Units 3 and 4 Diesel Fuel Oil 
    Testing Program, FPL will need to determine if the proposed program 
    change is at least as, if not more, effective, in detecting 
    unsatisfactory fuel oil. The EDGs will thus continue to function as 
    designed and the probability or consequences of previously evaluated 
    accidents will be unaffected.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed changes to the Technical Specifications will permit 
    the Technical Specification required testing of Emergency Diesel 
    Generator fuel oil using more recent editions of the American Society 
    for Testing and Materials (ASTM) standards currently listed in 
    Technical Specification Surveillance Requirements 4.8.1.1.2e. and 
    4.8.1.1.2f. Prior to changing the edition of the previously approved 
    ASTM standard being used to evaluate the EDG fuel oil, the proposed 
    edition standard will be evaluated pursuant to 10 CFR Sec. 50.59, 
    ``Changes, tests, and experiments.'' Title 10 CFR Sec. 50.59 permits a 
    licensee to make changes in the procedures as described in the safety 
    analysis report without prior Commission approval, provided that the 
    proposed changes does not involve an unreviewed safety question. Title 
    10 CFR Sec. 50.59(a)(2) states that a proposed change involves an 
    unreviewed safety question (ii) if a possibility for an accident or 
    malfunction of a different type than any evaluated previously in the 
    safety analysis report may be created. Consequently, since any change 
    to the edition of the ASTM standard to be used to evaluate EDG fuel oil 
    acceptability must be evaluated relative to the more restrictive 
    evaluation criterion of 10 CFR Sec. 50.59, then operation of the 
    facility in accordance with the proposed amendments would not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        ACTION statement g. of TS 3.8.1.1 is added to address the required 
    action in the event the new fuel oil properties do not meet the Diesel 
    Fuel Oil Testing Program limits. A failure to meet the API gravity, 
    kinematic viscosity, flash point or clarity limits is cause for 
    rejecting the new fuel oil prior to the addition to the Diesel Fuel Oil 
    Storage Tanks, but does not represent a failure to meet the Limiting 
    Condition for Operation (LCO) of TS 3.8.1.1, since the new fuel oil has 
    not been added to the storage tanks. Provided these new fuel oil 
    properties are met subsequent to the addition of the new fuel oil to 
    the storage tanks, 30 days is provided to complete the analyses of the 
    other fuel oil properties specified in Table 1 of ASTM-D975-81, except 
    sulfur which may be performed in accordance with ASTM-D1552-79 or ASTM-
    D2622-82. In the event the other new fuel oil properties specified in 
    Table 1 of ASTM-D975-81 are not met, ACTION statement g. of TS 3.8.1.1 
    provides an additional 30 days to meet the Diesel Fuel Oil Testing 
    Program limits. This additional 30 day period is acceptable because the 
    fuel oil properties of interest, even if they are not within limits, 
    would not have an immediate effect on EDG operation.
        ACTION statement h. of TS 3.8.1.1 is added to address the required 
    action in the event the stored fuel oil total particulates does not 
    meet the Diesel Fuel Oil Testing Program limits. Fuel oil degradation 
    during long term storage shows up as an increase in particulate, due 
    mostly to oxidation. The presence of particulate does not mean the fuel 
    oil will not burn properly in a diesel engine. The frequency for 
    performing surveillance on stored fuel oil is based on stored fuel oil 
    degradation trends which indicate that particulate concentration is 
    unlikely to change significantly between surveillances.
        Prior to changing the Turkey Point Units 3 and 4 Diesel Fuel Oil 
    Testing Program, FPL will need to determine if the proposed program 
    change is at least as, if not more, effective, in detecting 
    unsatisfactory fuel oil. Since the proposed changes do not involve a 
    change in the design of any plant system or component, and since the 
    proposed changes will need to evaluate the effect of any ASTM standard 
    edition change on the level of EDG reliability, the change proposed 
    will not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The proposed changes to the Technical Specifications will permit 
    the Technical Specification required testing of Emergency Diesel 
    Generator (EDG) fuel oil using more recent editions of the American 
    Society for Testing and Materials (ASTM) standards currently listed in 
    Technical Specification Surveillance Requirements 4.8.1.1.2e. and 
    4.8.1.1.2f. Prior to changing the edition of the previously approved 
    ASTM standard being used to evaluate the EDG fuel oil, the proposed 
    edition standard will be evaluated pursuant to 10 CFR Sec. 50.59, 
    ``Changes, tests, and experiments.'' Title 10 CFR Sec. 50.59 permits a 
    licensee to make changes in the procedures as described in the safety 
    analysis report without prior NRC approval, provided that the proposed 
    changes does not involve an unreviewed safety question. Title 10 CFR 
    Sec. 50.59(a)(2) states that a proposed change involves an unreviewed 
    safety question (iii) if the margin of safety as defined in the basis 
    for any technical specification is reduced. Consequently, since any 
    change to the edition of the ASTM standard to be used to evaluate EDG 
    fuel oil acceptability must be evaluated relative to the more 
    restrictive evaluation criterion of 10 CFR Sec. 50.59, then operation 
    of the facility in accordance with the proposed amendments would not 
    involve a significant reduction in a margin of safety.
        ACTION statement g. of TS 3.8.1.1 is added to address the required 
    action in the event the new fuel oil properties do not meet the Diesel 
    Fuel Oil Testing Program limits. A failure to meet the API gravity, 
    kinematic viscosity, flash point or clarity limits is cause for 
    rejecting the new fuel oil prior to the addition to the Diesel Fuel Oil 
    Storage Tanks, but does not represent a failure to meet the Limiting 
    Condition for Operation (LCO) of TS 3.8.1.1, since the new fuel oil has 
    not been added to the storage tanks. Provided these new fuel oil 
    properties are met subsequent to the addition of the new fuel oil to 
    the storage tanks, 30 days is provided to complete the analyses of the 
    other fuel oil properties specified in Table 1 of ASTM-D975-81, except 
    sulfur which may be performed in accordance with ASTM-D1552-79 or ASTM-
    D2622-82. In the event the other new fuel oil properties specified in 
    Table 1 of ASTM-D975-81 are not met, ACTION statement g. of TS 3.8.1.1 
    provides an additional 30 days to meet the Diesel Fuel Oil Testing 
    Program limits. This additional 30 day period is acceptable because the 
    fuel oil properties of interest, even if they are not within limits, 
    would not have an immediate effect on EDG operation.
        ACTION statement h. of TS 3.8.1.1 is added to address the required 
    action in the event the stored fuel oil total particulates does not 
    meet the Diesel Fuel Oil Testing Program limits. Fuel oil degradation 
    during long term storage shows up as an increase in particulate, due 
    mostly to oxidation. The presence of particulate does not mean the fuel 
    oil will not burn properly in a diesel engine. The frequency for 
    performing surveillance on stored fuel oil is based on stored fuel oil 
    degradation trends which indicate that particulate concentration is 
    unlikely to change significantly between surveillances.
        Prior to changing the Turkey Point Units 3 and 4 Diesel Fuel Oil 
    Testing Program, FPL will need to determine if the proposed program 
    change is at least as, if not more, effective, in detecting 
    unsatisfactory fuel oil. Since the proposed changes will require a 
    safety evaluation to assure that the reliability of the EDGs using fuel 
    oil tested in accordance with the different ASTM standard edition 
    maintains the current margin of safety, the proposed changes do not 
    involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
        Attorney for licensee: Harold F. Reis, Esquire, Newman and Holtzer, 
    P.C., 1615 L Street, NW., Washington, DC 20036.
        NRC Project Director: Mohan C. Thadani, Acting.
    
    Florida Power Corporation, et al.
    
    Docket No. 50-302
    
        Crystal River Nuclear Generating Plant, Unit No. 3, Citrus County, 
    Florida.
        Date of amendment request: September 30, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Crystal River 3 (CR3) Nuclear generating Plant Technical 
    Specifications (TS) to allow an increase in the rated thermal power 
    (RTP) for CR-3 from the current 2544 level to 2568 Megawatt thermal 
    (Wt). Accordingly, in TS 1.1, ``Definitions,'' would be revised to 
    indicate the new power level of 2568 MWt. The proposed change would not 
    require any hardware modifications.
        Basis for proposed no significant hazards consideration 
    determination: Currently, CR-3 is operating at a maximum RTP of 2544 
    MWt. The licensee proposes to operate at a maximum RTP of 2568 MWt, an 
    increase of 24 MWt over the current licensed power of 2544 MWt.
        The licensee states that the Babcock and Wilcox (B&W) 177 Fuel 
    Assembly (FA) Nuclear Steam Supply System (NSSS) in the CR3 design is 
    capable of operating at a thermal power level of 2772 MWt. Due to 
    limitations in the secondary area of the plant, the licensee requests 
    authorization to operate at 2568 MWt which is less than the design 
    level of 2772 MWt. The licensee performed a detailed engineering study 
    on this power increase.
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the probability 
    of occurrence or consequences of an accident previously evaluated. The 
    thermal-hydraulic and nuclear characteristics of the reactor core were 
    originally designed for a rated thermal power of 2568 MWt or higher. 
    Therefore, the proposed thermal power increase to the reference power 
    level of 2568 MWt does not change the original design assumptions and 
    analyses for the reactor core. Most of the design basis accidents and 
    transients were originally evaluated at the proposed power level. As 
    described more fully in this submittal, those transients and accidents 
    that were not originally evaluated at 2568 MWt were re-evaluated using 
    CR-3 FSAR [Final Safety Analysis Report] Chapter 14 accident sequence 
    of events, reactor protection criteria, and approved calculational 
    methods. Based on this evaluation and initial plant design evaluations, 
    FPC [Florida Power Corporation, the licensee for CR3] has determined 
    that the probability and consequences of design basis transients and 
    accidents are not significantly increased and that the radiological 
    consequences from the design basis transients and accidents remain well 
    below 10 CFR 100 limits.
        FPC has also reviewed CR-3 balance of plant and safety related 
    systems to determine which systems and components could be affected by 
    the proposed power increase. The changes to the reactor coolant system 
    and secondary conditions and parameters are discussed in this 
    submittal. These changes are minor in nature. The only Technical 
    Specification change is to revise the reference power to 2568 MWt. No 
    facility modifications will be required. FPC evaluated the systems and 
    components and concluded that these systems and components will 
    continue to perform within their design parameters with the unit 
    operating at 2568 MWt.
        Based on the foregoing, the proposed amendment does not 
    significantly increase the probability or consequences of an accident 
    previously evaluated.
        2. The proposed thermal power increase does not create the 
    possibility of a new or different kind of accident from previously 
    evaluated accidents. As noted above, the thermal-hydraulic and nuclear 
    characteristics of the reactor core were originally designed for 
    operation at the proposed thermal power. Therefore, operation at the 
    proposed power level does not introduce new or different performance 
    characteristics that create the possibility of a new or different kind 
    of accident.
        FPC has also reviewed CR-3 safety-related systems and balance of 
    plant systems to determine which systems could be affected by the 
    proposed power increase and the resultant minor changes in plant 
    parameters and operating conditions. Systems that could be affected 
    were evaluated using the licensing basis criteria described in the CR-3 
    FSAR to assure their adequacy at the increased power level. Included in 
    these evaluations were plant features that are not power level related 
    or directly affected by an increase in power level, as well as, 
    associated issues such as environmental considerations. Equipment 
    performance and plant operation were evaluated with respect to actual 
    performance versus projected operating conditions to identify any 
    hardware modifications required to achieve the upgraded power. Based on 
    this evaluation, FPC has determined that all systems will continue to 
    perform within their design parameters at 2568 MWt and that no physical 
    modifications to these systems will be necessary to accommodate a 2568 
    MWt rating. Only minor re-calibration of plant instrumentation to 
    reflect the increased power will be needed. The proposed power level 
    does not introduce any new performance characteristics or modes of 
    operation for plant systems and components, and does not introduce any 
    new failure modes.
        Based on the foregoing, the proposed amendment does not create the 
    possibility of a new or different kind of accident.
        3. The proposed amendment does not involve a significant reduction 
    in a margin of safety. The thermal-hydraulic and nuclear 
    characteristics of the reactor core were originally designed for 
    operation at the proposed power level. Most of the design basis 
    transients and accidents were originally analyzed assuming a power 
    level of 2568 MWt or higher. As described more fully in this submittal, 
    those transients and accidents that were not originally analyzed at 
    2568 MWt were re-evaluated using CR-3 FSAR Chapter 14 accident sequence 
    of events, reactor protection criteria, and approved calculational 
    methods. FPC has determined that operation with the proposed thermal 
    power will be bounded by the original analyses. In addition, FPC's 
    evaluation of affected plant systems and components revealed that plant 
    systems and components will continue to operate within their design 
    parameters with no significant change in a margin of safety.
        Based on the foregoing, the proposed amendment does not involve a 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629
        Attorney for licensee: A. H. Stephens, General Counsel, Florida 
    Power Corporation, MAC-A5D, P. O. Box 14042, St. Petersburg, Florida 
    33733.
        NRC Project Director: Mohan C. Thadani, (Acting).
    
    Indiana Michigan Power Company
    
    Docket Nos. 50-315 and 50-316
    
        Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan.
        Date of amendment request: August 3, 1994.
        Description of amendment requests: The proposed amendments would 
    allow the radiological effluent technical specifications (TS) to be 
    relocated to other controlled documents. Procedural details contained 
    in the current radiological effluents TS have been relocated to either 
    the Offsite Dose Calculation Manual (OCDM) or the Process Control 
    Program (PCP), as applicable. Proposed revisions to the OCDM and PCP 
    have been prepared in accordance with the proposed changes to the 
    administrative controls section of the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1
        The changes described above in no way negatively impact the 
    requirements of the T/Ss. Separating the turbine room sump releases 
    from the others is purely a clarification of the method we handle 
    releases. The six ground monitoring wells added to the T/S table 
    updates our current monitoring practice. With the six extra wells to 
    monitor, we exceed the monitoring requirements of the T/Ss. Therefore, 
    it is concluded that the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        Criterion 2
        No changes to the LCOs for either T/S are proposed as part of this 
    amendment request. The proposed change does not involve any physical 
    changes to the plant or any changes to plant operations. The changes 
    merely propose to update our methods of implementing the T/S with our 
    current practices. Thus, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Criterion 3
        The changes described above in no way negatively impact the 
    requirements of the T/Ss. Separating the turbine room sump releases 
    from the others is purely a clarification of the method we handle 
    releases. The six ground monitoring wells added to the T/S table 
    updates our current monitoring practice. With the extra wells to 
    monitor, we exceed the monitoring requirements called for in the T/Ss. 
    Therefore, it is concluded that the proposed changes do not involve a 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Niagara Mohawk Power Corporation
    
    Docket No. 50-410
    
        Nine Mile Point Nuclear Station, Unit 2, Oswego County, New York.
        Date of amendment request: October 5, 1994.
        Description of amendment request: The proposed license amendment 
    would revise the applicability requirements of Technical Specification 
    (TS) 3.7.3 to require operability of the Control Room Outdoor Air 
    Special Filter Train System in Operational Conditions 1, 2, 3 and ** 
    (when irradiated fuel is being handled in the reactor building and 
    during CORE ALTERATIONS and operations with a potential for draining 
    the reactor vessel and uncovering irradiated fuel) rather than in all 
    Operational Conditions and * * *. The applicability requirements for 
    Action Statement b of TS 3.7.3 and for the Radiation Monitoring 
    Instrumentation required operable by TS Tables 3.3.7.1-1 and 4.3.7.1-1 
    would be changed in a similar manner. The proposed amendment would also 
    add a notation to Action Statement b.1 of TS 3.7.3 stating that the 
    provisions of Specification 3.0.4 are not applicable provided an 
    operable control room filter train is in the emergency pressurization 
    mode of operation. The licensee stated that these proposed changes are 
    consistent with the requirements of the NRC's Improved Standard 
    Technical Specifications (NUREG-1433) and with Generic Letter 87-09, 
    ``Section 3.0 and 4.0 of the Standard Technical Specifications (STS) on 
    the Applicability of Limiting Conditions for Operation and Surveillance 
    Requirements.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The Control Room Outdoor Air Special Filter Train System is not an 
    initiator or precursor to an accident. The Control Room Outdoor Air 
    Special Filter Train System responds to a release of radioactivity to 
    the outside environment as detected in the air supply to the control 
    room by providing a radiologically controlled environment within the 
    control room. In operational conditions 4 and 5, the probability and 
    consequences of a design basis accident are reduced due to the pressure 
    and temperature limitations in these operational conditions. Therefore, 
    maintaining the chiller subsystem operable is not required in 
    operational conditions 4 and 5, except for the * * * operational 
    condition. Therefore, a change to applicability and action statements 
    of LCO [Limiting Condition For Operation] 3.7.3 cannot affect the 
    probability of a previously evaluated accident.
        All accidents which take credit for operation of the Control Room 
    Outdoor Air Special Filter Train System in the emergency pressurization 
    mode of operation are analyzed and presented in Chapter 15 of the USAR 
    [Updated Safety Analysis Report]. These accidents can only occur in 
    operational conditions 1, 2, 3 and * * *.
        Accordingly, the proposed change in the applicability of LCO 3.7.3 
    from all operational conditions (i.e., 1, 2, 3, 4, 5 and * * *) to 
    operational conditions 1, 2, 3 and * * * does not significantly 
    increase the consequences of an accident previously evaluated. The 
    proposed change to action statement b of LCO 3.7.3 and to Tables 
    3.3.7.1-1 and 4.3.7.1-1 of LCO 3.3.7.1 is consistent with the above 
    change.
        Sections 15.7.4 and 15.7.5 of the USAR evaluate a fuel handling 
    accident and a spent fuel cask drop accident, respectively. The 
    radiological evaluation of these accidents considers the unfiltered 
    radioactivity that enters the control room prior to the automatic 
    operation of the Control Room Outdoor Special Filter Train System in 
    the emergency pressurization mode of operation. The radiological 
    consequences of these accidents are within the limits of GDC [General 
    Design Criterion]-19.
        With one control room filter train inoperable and prior to entering 
    the operational condition, the proposed change to action statement b.1 
    of LCO 3.7.3 would require an operable control room filter train be 
    placed in the emergency pressurization mode of operation. During an 
    accident involving the release of radioactivity to the environment, an 
    operable control room filter train would already be running in the 
    emergency pressurization mode and performing its safety function, 
    thereby preventing the entry of unfiltered radioactivity into the 
    control room. Therefore, if a fuel handling accident or a spent fuel 
    cask drop accident were to occur and release radioactivity, the control 
    room personnel radiological doses would be less than the doses depicted 
    in the USAR. Accordingly, the Technical Specification change to action 
    statement b.1 does not significantly increase the consequences of a 
    previously evaluated accident.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        This amendment does not involve any accident precursors or 
    initiators. In addition, this amendment does not require any changes to 
    plant equipment.
        During an accident involving the release of radioactivity to the 
    environment an operable control room filter train would already be 
    running in the emergency pressurization mode and performing its safety 
    function. Furthermore, the operating status of a running control room 
    filter train would be unaffected by the receipt of an automatic start 
    signal due to high radiation in either air intake to the Control Room 
    Outdoor Air Special Filter Train System. Therefore, the proposed 
    amendment will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed change in the applicability of LCO 3.7.3 from all 
    operational conditions (i.e., 1, 2, 3, 4, 5 and * * *) to operational 
    conditions 1, 2, 3 and * * * is consistent with the safety analysis 
    contained in the USAR. The proposed changes to action statement b of 
    LCO 3.7.3 and to Tables 3.3.7.1-1 and 4.3.7.1-1 of LCO 3.3.7.1 is 
    consistent with the above change.
        Entry into the ** operational condition for LCO 3.7.3 with one 
    control room filter train inoperable and the other control room filter 
    train operable and operating in the emergency pressurization mode 
    provides a comparable level of safety to two operable non-running 
    control room filter trains. The remedial measure prescribed by 
    Technical Specification action statement b.1 (placing an operable 
    control room filter train in the emergency pressurization mode of 
    operation) for which the exception to LCO 3.0.4 is proposed provides a 
    sufficient level of protection to permit operational mode changes and 
    safe long-term operation of NMP2 [Nine Mile Point Unit 2] consistent 
    with the licensing basis described in the USAR. Therefore, the proposed 
    change to action statement b.1 is consistent with Generic Letter 87-09, 
    ``Sections 3.0 and 4.0 of the Standard Technical Specifications (STS) 
    on the Applicability of Limiting Conditions for Operation and 
    Surveillance Requirements.'' Accordingly, this change will not 
    significantly reduce the margin of safety.
        This proposed amendment is consistent with the Improved Standard 
    Technical Specifications, NUREG-1433. Accordingly, as determined by the 
    analysis above, this proposed amendment involves no significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Ledyard B. Marsh.
    
    Niagara Mohawk Power Corporation
    
    Docket No. 50-410
    
        Nine Mile Point Nuclear Station, Unit 2, Oswego County, New York.
        Date of amendment request: October 21, 1994.
        Description of amendment request: The proposed amendment would add 
    a footnote to Technical Specification (TS) 4.8.1.1.2.e.8 which would 
    permit performance of the 24-hour functional test of the emergency 
    diesel generators (EDGs) during power operation. TS 4.8.1.1.2.e.8 
    currently requires the 24-hour functional test of the EDGs be performed 
    at least once per 18 months during shutdown; the proposed amendment 
    would permit this testing to be performed during power operation 
    provided the other two EDGs are operable. If either of the other two 
    EDGs become inoperable, the test would be aborted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change to permit the 24 hour functional test of the 
    diesels to be performed during power operation does not increase the 
    chances for a previously analyzed accident to occur. The function of 
    the diesels is to supply emergency power in the event of a loss of 
    offsite power. Operation of the diesels is not a precursor to any 
    accident. Furthermore, the diesel generator being tested will remain 
    operable and will be available to supply emergency loads within the 
    required time. In addition, the two remaining diesel generators will be 
    operable during the test. Consequently, if an offsite disturbance were 
    to occur that affected the operability of the diesel being tested, the 
    two remaining diesels would be capable of feeding the loads necessary 
    for safe shutdown of the plant. This addresses the concerns raised in 
    Information Notice 84-69 regarding the operation of emergency diesel 
    generators connected in parallel with offsite power. In summary, the 
    proposed changes do not adversely affect the performance or the ability 
    of the diesel generators to perform their intended function.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The proposed amendment to the 24 hour functional surveillance test 
    will not affect the operation of any safety system or alter its 
    response to any previously analyzed accident. The diesel will 
    automatically transfer from the test mode if necessary to supply 
    emergency loads in the requried time. The test mode is used for the 
    monthly surveillance of the diesel generators as well, therefore, no 
    new plant operating modes are introduced. In the event the diesel fails 
    the functional test it will be declared inoperable and the actions 
    required for an inoperable diesel will be performed. The remaining two 
    diesel generators will be operable and are capable of feeding the loads 
    necessary for safe shutdown of the plant.
        Therefore, the proposed change will not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed amendment will not reduce availability of the diesel 
    generator being tested to provide emergency power in the event of a 
    loss of offsite power. If a loss of offsite power or a loss of coolant 
    accident occurs during the surveillance test, the emergency bus would 
    de-energize and shed load. The diesel generator would then transfer 
    from the test mode to the emergency mode. It would then be available to 
    automatically supply emergency loads. In addition, the two remaining 
    generators will be operable during the test. Consequently, if an 
    offsite disturbance were to occur that affected the operability of the 
    diesel begin tested, the two remaining diesels would be capable of 
    feeding the loads necessary for safe shutdown of the plant. The time 
    required for the diesel being tested to pick up emergency loads will 
    not be affected by performing the 24 hour functional test during power 
    operation.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Ledyard B. Marsh.
    
    Northeast Nuclear Energy Company et al.
    
    Docket No. 50-336.
    
        Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut.
        Date of amendment request: October 18, 1994.
        Description of amendment request: The proposed amendment would 
    require three type A overall Integrated Containment Leakage Tests be 
    conducted at approximately equal intervals during shutdowns during each 
    10-year service period. For the third Type A test for the second 10-
    year period, it would be conducted during the thirteenth refueling 
    outage extending the second 10-year service period to the end of the 
    thirteenth refueling outage. The amendment would also change the 
    Containment Leakage Bases by reflecting the conditions of a proposed 
    exemption to 10 CFR 50, Appendix J, that would remove the requirement 
    that the third Type A test for each 10-year period be conducted when 
    the plant is shutdown for the 10-year plant inservice inspection.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        * * * The proposed changes do not involve a SHC [significant 
    hazards consideration] because the change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        Type A tests are performed to ensure that the total leakage from 
    containment does not exceed the maximum allowable primary containment 
    leakage rate at the design pressure. This ensures compliance with the 
    dose limits of 10 CFR 100.
        The proposal to revise Surveillance Requirement 4.6.1.2.a of the 
    Millstone Unit No. 2 Technical Specifications will increase the 
    flexibility for scheduling the Type A tests. It does not modify the 
    maximum allowable leakage rate at the design containment pressure, does 
    not impact the design basis of the containment, and does not make any 
    physical or operational changes to existing plant structures, systems, 
    or components.
        The first two Type A tests of the second 10-year service period for 
    Millstone Unit No. 2 have been conducted. The results of these tests 
    demonstrate that Millstone Unit No. 2 has maintained control of 
    containment integrity by maintaining margin between the acceptance 
    criterion and the ``As-Found'' and ``As-Left'' leakage rates.
        Historically, Type A tests have a relatively low failure rate where 
    Type B and C testing (local leakage rate tests) could not detect the 
    leakage path. Most Type A test failures are attributed to failures to 
    Type B or C components (containment penetrations and isolation valves). 
    Type B and C components are tested per Surveillance Requirement 
    4.6.1.2.d for the Millstone Unit No. 2 Technical Specifications. These 
    tests are required to be conducted at intervals no greater than 24 
    months, and the acceptance criterion for the combined leakage rate for 
    all penetrations and valves subject to the Type B and C tests is 0.6 
    La. These local leakage rate tests provide assurance that 
    containment integrity is maintained. The relatively low ``As-Left'' 
    Type B and C total leakage resulting from the past outage indicates 
    that the leakage has been maintained within the technical specification 
    acceptance criterion. The Type B and C tests will continue to be 
    performed in accordance with the requirements of Surveillance 
    Requirement 4.6.1.2.d. However, on September 26, 1994, NNECO submitted 
    a request for a one-time technical specification change, request for 
    enforcement discretion, and a request for a scheduler exemption from 
    Appendix J to 10 CFR 50 regarding the Schedule for Type B and C 
    testing. The NRC verbally granted enforcement discretion on September 
    24, 1994, and written enforcement discretion on September 30, 1994. The 
    schedular exemption request was granted on October 12, 1994.
        The previous Type A, B, and C tests demonstrate that Millstone Unit 
    No. 2 has maintained control of containment integrity by maintaining a 
    conservative margin between the acceptance criterion and the ``As-
    Found'' and ``As-Left'' leakage results. Based on this, the Millstone 
    Unit No. 2 containment is considered to be in sound condition. No 
    operations are known to have occurred which would suggest any 
    substantial degradation of these results.
        Based on the above, the proposal to revise Surveillance Requirement 
    4.6.1.2.a of the Millstone Unit No. 2 Technical Specifications does not 
    involve a significant increase in the probability or consequences of an 
    accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposal to revise Surveillance Requirement 4.6.1.2.a of the 
    Millstone Unit No. 2 Technical Specifications will increase the 
    flexibility in scheduling the Type A tests. It does not make any 
    physical or operational changes to existing plant structures, systems, 
    or components. In addition, the proposal does not modify the acceptance 
    criterion for the Type A tests. Maintaining the leakage through the 
    containment boundary to the atmosphere within a specific value ensures 
    that the plant complies with the requirements of 10 CFR 100. The 
    containment boundary serves as an accident mitigator; it is not an 
    accident initiator. Therefore, the proposal to revise Surveillance 
    Requirement 4.6.1.2.a does not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        The proposal to revise Surveillance Requirement 4.6.1.2.a of the 
    Millstone Unit No. 2 Technical Specifications will increase the 
    flexibility for scheduling the Type A tests. It does not modify the 
    maximum allowable leakage rate at the design containment pressure, does 
    not impact the design basis of the containment, and does not make any 
    physical or operational changes to existing plant structures, systems, 
    or components.
        The first two Type A tests of the second 10-year service period for 
    Millstone Unit No. 2 have been conducted. The results of these tests 
    demonstrate that Millstone Unit No. 2 has maintained control of 
    containment integrity by maintaining margin between the acceptance 
    criterion and the ``As-Found'' and ``As-Left'' leakage rates. 
    Additionally, the results of the last Type B and C tests had 
    significant margin with respect to the acceptance criterion. Based on 
    the previous Type A, B, and C tests, the Millstone Unit No. 2 
    containment is considered to be in sound condition. No operations are 
    known to have occurred which would suggest any substantial degradation 
    of these results.
        Based on the above, the proposal does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al.
    
    Docket No. 50-423
    
        Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut.
        Date of amendment request: September 30, 1994.
        Description of amendment request: The licensee has proposed to 
    revise the Technical Specifications (1) to clarify the definition of 
    core alterations, (2) to change the verbiage in the Limiting Condition 
    For Operation (LCO) addressing the refueling operations, (3) to make 
    changes to three surveillance requirements involving source range 
    instrumentation, and (4) to change the LCO regarding the Residual heat 
    Removal and coolant circulation water levels to be consistent with the 
    guidance provided in NUREG-1431.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve an SHC [significant hazards 
    consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Boron Dilution in Mode 6--A boron dilution in Mode 6 is precluded 
    by technical specification requirements to close and lock all dilution 
    source valves. There is a provision for dilution valves to be opened 
    under administrative controls; in this case, cautionary measures will 
    be taken to control and monitor the reactivity addition. Deletion of 
    the source range analog operational test prior to core alterations will 
    not impact an accident previously evaluated since the sources range 
    monitors are verified operable prior to entry into Mode 6 and every 7 
    days thereafter. The change in definition for a core alteration means 
    that components which do not effect reactivity may be moved within the 
    reactor vessel without any additional condition such as direct 
    supervision of an SRO.
        Since a boron dilution would not be initiated by movement of 
    nonfuel components within the reactor vessel, it is not impacted by the 
    change in definition of a core alteration.
        Inadvertent Loading of a Fuel Assembly--Movement of a fuel assembly 
    would be performed as a core alteration under the supervision of an 
    SRO, therefore, it would not be impacted by the change to the 
    definition of a core alteration. The change to the source range 
    monitors also will not affect the probability of occurrence of a 
    misloaded fuel assembly since this accident is precluded by 
    administrative controls, as well as the source range monitors. Also, 
    there will be no degradation in the reliability or accuracy of the 
    source range monitors due to this change. The deletion of the 
    requirement to perform the analog channel operational test within eight 
    hours prior to core alterations will not impact performance of the 
    monitors, since they have to be checked prior to entry into Mode 6 and 
    every 7 days thereafter.
        Fuel Handling Accident--Movement of fuel will not affect this 
    accident, because it will still be considered a core alteration. 
    Therefore, there is no effect on the probability of a fuel handling 
    accident. The source range monitors are not involved in the occurrence 
    of a fuel handling accident. The fuel handling accident is the only 
    accident considered here with radiological consequences. It will not be 
    impacted by the proposed changes.
        Loss of RHR in Mode 6--The probability of this accident will not be 
    changed since the new requirement is the same as before. As before, RHR 
    may be secured for up to one hour per eight-hour period and boron 
    dilution operations may not be performed with RHR secured (although 
    this requirement is being added to the notes, the requirement is also 
    given elsewhere in the technical specifications). Additionally, the 
    existing reactor coolant system (RSC) temperature limits must still be 
    met.
        Based on the above, the proposed changes do not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        All required systems will continue to operate as before. Therefore, 
    there is no possibility of a new or different kind of accident. The 
    deletion of the source range analog channel operational test within 
    eight hours prior to core alterations will not affect the performance 
    of the monitors since they will have had this test completed prior to 
    entry into Mode 6 and every 7 days thereafter. The change in definition 
    of a core alteration cannot create the possibility of a new type of 
    accident because those initiating events for accidents will remain 
    classified as core alterations.
        3. Involve a significant reduction in the margin of safety.
        The margin of safety for the above listed accidents will remain as 
    before.
        a. Boron dilution in Mode 6--This accident calculates the time from 
    receipt of a shutdown margin monitor dilution alarm until the core 
    reaches criticality. Since this time is not changed, there is no 
    reduction in the margin of safety. In this case, the dilution is 
    precluded by administrative controls which will not be impacted by the 
    proposed changes.
        b. Inadvertent Loading of a Fuel Assembly--Technical Specification 
    3.9.1.1 protects against this accident by requiring sufficient boron in 
    the RCS to prevent criticality for any core configuration including two 
    stuck RCCAs [rod cluster control assemblies] in the fully withdrawn 
    position. Since this requirement will not change, the margin of safety 
    will not change.
        c. Fuel Handling Accident--The margin of safety for the 
    radiological limits is not changed.
        d. Loss of RHR--Changes are editorial due to the revised definition 
    of a core alteration. There is no change to the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L.M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northern States Power Company
    
    Docket Nos. 50-282 and 50-306
    
        Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota.
        Date of amendment requests: October 3, 1994.
        Description of amendment requests: The proposed amendment would 
    revise Prairie island Nuclear Generating Plant Technical Specification 
    4.6, ``Periodic Testing of Emergency Power Systems.'' Specifically, the 
    proposed amendment would modify the emergency diesel generator (EDG) 
    24-hour load test requirements to provide a indicated load range of 
    103-110% of the continuous rating. The proposed amendment would also 
    rephrase various EDG test requirements to provide clarity and delete 
    the requirement to verify that the auto-connected loads do not exceed 
    3000 kw (Unit 2 5100kw).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        Changing the specification from ``unit'' to ``diesel generator'' 
    does not change the intent of the specification, it merely clarifies 
    the original intent and therefore cannot involve a change in the 
    probability or consequences of an accident.
        Changing the 22-hour lower range limit from a load of 90% to an 
    indicated load of 92% removes possible ambiguity from the specification 
    but does not change the actual requirement, therefore it cannot involve 
    a change in the probability or consequences of an accident.
        Removing the 22-hour upper range limit from the specification does 
    not reduce the conservatism of the test since operating at a higher 
    load provides more evidence of the ability of the machine to carry the 
    accident loads. For this reason, this change will not involve any 
    increase in the consequences of an accident. Also, increasing the load 
    at which the diesel generator is tested cannot affect the probability 
    of an accident.
        The NRC staff has pointed out, in Generic Letter 88-15, the hazards 
    of testing the Diesel Generator at a load greater than the design 
    rating. The proposed change is intended to ensure that the design 
    rating is not inadvertently exceeded. Since the recent installation of 
    two additional emergency diesel generators, the highest anticipated 
    event loads are: Unit 1-2414kW, Unit 2-3813 kW. For these diesel 
    generators, then, 103% of the continuous ratings:
         Unit 1, 103% of 2750 kW (continuous rating) = 2832.5 kW 
    represents 117.3% of the highest anticipated event load and;
         Unit 2, 103% of 5400 kW (continuous rating) = 5562 kW 
    represents 145.9% of the highest anticipated event load.
        A test load of 103%, therefore would still be significantly greater 
    than the load required during accident conditions. Since an adequate 
    level of electrical load carrying capacity of the diesel generators 
    (and thus their accident mitigating functions) would still be 
    demonstrated by the surveillance test, the consequences of an accident 
    would be unaffected by the proposed change. The probability of 
    occurrence of a previously evaluated accident would be unaffected since 
    testing a diesel generator at load between 103 and 110 percent instead 
    of at load between 105 and 110 percent could not cause or contribute to 
    the initiation of an accident. For these reasons, this change could 
    have no effect on the probability or consequences of an accident 
    previously evaluated.
        Allowing momentary transients outside of the test band does not 
    affect the conduct of the test, it merely allows momentary swing 
    outside the specified band to not invalidate the test. Not allowing 
    momentary transients would not prevent them, it would only require 
    conducting the test longer until the specified time period was achieved 
    without moving outside the band. Since the machine will not be operated 
    any differently, this specification change cannot affect the 
    probability or consequences of an accident previously evaluated.
        Proposed changes A, B, C, D, and the first part of E [identified as 
    such in the submittal] are intended to clarify the meaning of the 
    existing specifications without changing the requirements. For this 
    reason, these proposed changes to the Technical Specifications will not 
    change the manner in which the plant is operated or maintained. These 
    administrative changes, therefore, will effect on the probability or 
    consequences of an accident previously evaluated.
        The second part of E (verification of the bypass of diesel 
    generator trips during a simulated safety injection signal vs 
    concurrent safety injection and loss of offsite power signals) does not 
    change the intended function which is to be tested but, rather, reduces 
    the special conditions (temporary electrical jumpers to simulate the 
    loss of offsite power) in which the plant needs to be placed in order 
    to perform the test.
        Proposed change F (removal of the verification that the auto-
    connected load do not exceed 3000 or 5100 kW) does not reduce the 
    assurance of the ability of the diesel generators to perform the 
    accident mitigation functions since this verification is performed by 
    other, more pertinent, means.
        Therefore, these changes cannot increase the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment will not create the possibility of a new 
    or different king of accident from any accident previously analyzed.
        Changing the specification from ``unit'' to ``diesel generator'' 
    does not change the intent of the specification, it merely clarifies 
    the original intent and therefore cannot create the possibility of a 
    new or different kind of accident.
        Changing the 22-hour lower range limit from a load of 90% to an 
    indicated load of 92% removes possible ambiguity from the specification 
    but does not change the actual requirement.
        Removing the 22-hour upper range limit from the specification does 
    not change the manner in which the surveillance is performed. It only 
    affects whether the time spent above 100% load can be counted toward 22 
    hours in the 22-hour portion of the test. This change would not allow 
    any new modes of operation nor does it allow any modification to the 
    plant.
        As stated above, testing a diesel generator at a load between 103 
    and 110% instead of between 105 and 110% could not cause or contribute 
    to the initiation of an accident.
        Allowing momentary transients outside of the test band does not 
    affect the conduct of the test, it merely allows momentary swings 
    outside the specified band to not invalidate the test. Not allowing 
    momentary transients would not prevent them, it would only require 
    conducting the test longer until the specific time period was achieved 
    without moving outside the band.
        Therefore, for these reasons, operation of the facility in 
    accordance with the proposed amendment will not create the possibility 
    of a new or different kind of accident from any accident previously 
    analyzed.
        As stated above [for changes A-F], the proposed changes will not 
    cause a change in the way in which the plant is operated or maintained, 
    excepted for the reduction of the special conditions in which the plant 
    needs to be placed in order to test the bypass of the diesel generator 
    trips. Therefore, these administrative changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously analyzed.
        3. The proposed amendment will not involve a significant reduction 
    in a margin of safety.
        Changing the specification from ``unit'' to ``diesel generator'' 
    does not change the intent of the specification, it merely clarifies 
    the original intent and therefore cannot affect the margin of safety.
        Changing the 22-hour lower range limit from a load of 90% to an 
    indicated load of 92% removes possible ambiguity from the specification 
    but does not change the actual requirement and therefore cannot affect 
    the margin of safety.
        The margin of safety is not affected by removal of the 22-hour 
    upper range limit on the operation of the diesel generators during 
    surveillance testing since the margin of safety is related to the 
    magnitude of the accident loads and the maximum capacity of the machine 
    to carry load and this margin would be unaffected by this change.
        The capacity of each diesel generator to carry electrical load can 
    not be diminished by being tested at a lower load. Also, load testing 
    to less than 105% but more than 103% does not lessen the confidence in 
    the ability of the diesel generators to carry adequate load for this 
    facility since these diesel generators have significantly greater load 
    capacity than required by Standard Review Plan guidance in this regard 
    (the guidance allows peak accident load up to 100% of the continuous 
    rating versus Unit 1 diesel generators peak accident load of 87.8% and 
    Unit 2 diesel generators peak accident load of 70.6%). Therefore, this 
    change will not involve a significant reduction in the margin of 
    safety.
        Allowing momentary transients outside of the test band does not 
    affect the conduct of the test, it merely allows momentary swings 
    outside the specified band to not invalidate the test. Not allowing 
    momentary transients would not prevent them, it would only require 
    conducting the test longer until the specified time period was achieved 
    without moving outside the band. Since the machine will not be operated 
    any differently per the new specification, the margin of safety is 
    unaffected.
        As stated above [for changes A-F], the proposed changes will not 
    cause a change in the way in which the plant is operated or maintained, 
    except for the reduction of the special conditions in which the plant 
    needs to be placed in order to test the bypass of the diesel generator 
    trips. Therefore, these administrative change will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet mall, Minneapolis, 
    Minnesota 55401.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Omaha Public Power District
    
    Docket No. 50-285
    
        Fort Calhoun Station, Unit No. 1, Washington County, Nebraska.
        Date of amendment request: October 7, 1994.
        Description of amendment request: The proposed amendment to the 
    Technical Specifications (TSs) would (1) delete the surveillance 
    requirements contained in TS 3.6(3)a for the raw water backup valves to 
    the containment cooling coils, (2) delete the surveillance requirements 
    contained in TS 3.2, Table 3-5, item 6, for raw water valves, and (3) 
    revise the basis of TS 2.4 to reflect these changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The deletion of surveillance requirements contained in Technical 
    Specifications (TS) 3.2, Table 3-5, Items 6 and 3.6(3)a does not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        TS 3.6(3)a requires the Raw Water (RW) backup valves to the 
    containment air coolers to be tested each refueling outage. In 1990, 
    during the process of reviewing several open items created by the 
    design basis reconstitution project, an engineering analysis determined 
    that RW direct cooling of the containment air cooling coils should not 
    be used after an accident that has created elevated temperature 
    conditions inside containment. The high containment air temperatures, 
    in conjunction with the low back pressure in the containment cooling 
    coils when in the RW direct cooling mode, introduces the possibility of 
    vaporization inside the coils. Therefore, the use of RW direct cooling 
    for the containment air coolers has been discontinued in post-Loss of 
    Coolant Accident (LOCA) or post-Main Steam Line Break (MSLB) 
    situations. The issue of not being able to utilize RW direct cooling to 
    the containment air cooling coils was reported to the NRC in LER-90-25, 
    dated October 29, 1990 and LER-90-25 Revision 1, dated December 17, 
    1990.
        Raw water direct cooling of the containment air coolers is possible 
    if the containment atmospheric temperatures are less that 150 deg.F. If 
    RW direct cooling of the containment air coolers was utilized after a 
    LOCA or MSLB accident, it could only be used for long-term containment 
    atmospheric cooling. These conditions are essentially equivalent to 
    that associated with conditions in containment during normal plant 
    operation. RW direct cooling of the containment air coolers is not a 
    required post-accident function to maintain containment pressure below 
    60 psig. Since these valves are not required to perform a post-accident 
    function, deletion of the requirements to test these valves does not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        TS 3.2, Table 3-5, Item 6 requires that valves in the RW system be 
    tested every refueling outage. The valves tested by this surveillance 
    that could perform a safety function are already tested in accordance 
    with TS 3.3(1). Therefore testing of these valves under TS 3.2, Table 
    3-5, Item 6 is redundant to TS 3.3(1)a.
        (2) The proposed changes do not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        There will be no physical alterations to the plant configuration, 
    changes to setpoint values, or changes to the implementation of 
    setpoints or limits as a result of this proposed change. Valves that 
    are required to be repositioned during an accident to mitigate the 
    consequences will still be tested on a refueling frequency. The 
    proposed change only deletes unnecessary or redundant testing 
    requirements from the TS. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from any 
    previously analyzed.
        (3) The proposed changes do not involve a significant reduction in 
    a margin of safety.
        The proposed changes delete unnecessary or redundant surveillance 
    requirements within the TS. The deletion of TS 3.2, Table 3-5 Item 6, 
    only deletes testing requirements that are already required to be 
    conducted by TS 3.3(1)a. The deletion of the requirement to test the RW 
    backup valves to the containment air coolers in TS 3.6(3) only deletes 
    an unnecessary surveillance. RW direct cooling of the containment air 
    coolers is not required to maintain containment pressure below the 
    design limit of 60 psig. Therefore, the proposed changes do not involve 
    a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: LeBoeuf, Lamb, Leiby, and MacRae, 1875 
    Connecticut Avenue, N.W., Washington, D.C. 20009-5728.
        NRC Project Director: Theodore R. Quay.
    
    Pennsylvania Power and Light Company
    
    Docket Nos. 50-387 and 50-388
    
        Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania.
        Date of amendment request September 26, 1994.
        Description of amendment request: The amendment would remove the 
    requirement for operability of the Average Power Range Monitors (APRMs) 
    while the plant is in Operational Condition 5. However, the requirement 
    for the APRMs to be operable during a shutdown margin demonstration, 
    when the mode switch is in Startup, will remain unchanged.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    construction, which is presented below:
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Not requiring APRMs to be OPERABLE in OPCON 5 will not increase the 
    probability of inadvertent reactor critically during refueling 
    operations. Refueling Interlocks, NMS [Neutron Monitoring System] (SRMs 
    [Source Range Monitor], IRMs [Intermediate Range Monitor]), and 
    procedural restrictions provide assurance that inadvertent criticality 
    does not occur due to the simultaneous withdrawal or removal of two 
    control rods or due to the inadvertent insertion of a fuel bundle into 
    a core location with a control blade removed.
        The FSAR [Final Safety Analysis Report] Section 15.4.1 discusses 
    the potential for a control rod withdrawal error during refueling and 
    start-up operations. The discussion concludes that the withdrawal of 
    one control rod does not require a safety action because the total 
    worth of one control rod is not sufficient to cause criticality. The 
    attempted withdrawal of two control rods, assuming an operator error 
    and a single active failure, would result in a control rod block 
    initiated by the Refueling Interlocks. The safety-related IRM 
    subsystem, which is required by Technical Specifications to be OPERABLE 
    while in OPCON 5, is designed to generate a rod block or reactor scram 
    on high neutron flux and is therefore a backup protective system for 
    the Refueling Interlocks during refueling.
        The Safety-related IRM subsystem of the NMS is required by 
    Technical Specifications to be OPERABLE during OPCON 5 to support the 
    safety design bases of the NMS and RPS [Reactor Protection System]. The 
    SRM is not a safety-related subsystem but is important to plant safety 
    and is required by Technical Specifications to be OPERABLE in OPCON 5. 
    The SRM subsystem provides the plant operator with neutron flux levels 
    from startup conditions to the IRM operating range. The SRMs and IRMs 
    are designed to respond to local core conditions and would indicate and 
    respond (control rod block or scram) to an accident condition to 
    mitigate the transient. Thus, the APRMS are not necessary to be 
    OPERATOR in OPCON 5. The proposed Technical Specification change will 
    not alter the current requirements that the APRMs be OPERABLE during 
    shutdown margin demonstrations in OPCON 5 when the mode switch is in 
    Startup.
        The proposed Technical Specification change would reduce the APRM 
    operability requirement in OPCON 5 and would not affect the FSAR 
    evaluation of the inadvertent criticality due to the withdrawal or 
    removal of the highest worth control rod or due to the insertion of 
    fuel bundles in uncontrolled cells. The FSAR concludes that the 
    Refueling Interlocks and plant procedures provide assurance that 
    inadvertent criticality does not occur during refueling.
        The consequences of an accident will not be increased by the 
    proposed Technical Specification change because of the existing lines 
    of defense which prevent an inadvertent criticality event during 
    refueling, e.g., administrative restrictions, refueling procedures, 
    licensed plant operators, SRMs, Refueling Interlocks, and IRMs. 
    Furthermore, should the number of operator IRM or SRM channels be less 
    than that required by Technical Specifications, the Technical 
    Specifications require that core alteration activities be suspended and 
    all insertable control rods be inserted into the core.
        Therefore, the proposed changes do not result in an increase in the 
    probability or consequences of an accident previously evaluated.
        II. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes to the Technical Specifications will remove 
    the APRM operability requirement while in OPCON 5 (except for shutdown 
    margin demonstration testing); however, the SRMs and IRMs will still be 
    required to be OPERABLE in OPCON 5.
        The IRMs are safety-related and are designed to detect and respond 
    to increases in neutron flux within the local core regions. Any 
    inadvertent increases in neutron flux during refueling would originate 
    at a local core location, i.e., rod withdrawal error or fuel bundle 
    insertion. Technical Specifications require IRM operability and will 
    generate an RPS scram or control rod block if neutron flux increased to 
    the setpoint. Therefore, removing the APRMs operability requirement in 
    OPCON 5 would not effect any safety related equipment or equipment 
    important to safety.
        The APRMs provide core power information to the control room 
    operator and also provide trip signals to the RMCS [Reactor Manual 
    Control System] and RPS as required. The absence of an APRMs input 
    signal will not affect these systems during refueling operations.
        Removing the APRMs operability in OPCON 5 will not affect the 
    response of safety-related equipment as previously evaluated in the 
    FSAR. The proposed changes to the Technical Specifications do not 
    affect any safety-related equipment or equipment important to safety.
        The proposed changes to the Technical Specifications would remove 
    the APRMs operability requirement during refueling operations. 
    Technical Specifications require IRM operability and will generate an 
    RPS scram or control rod block if neutron flux increased to the 
    applicable setpoint.
        No new types of accidents would be introduced since the SRMs and 
    IRMs are available and required to be OPERABLE in OPCON 5. Both SRMs 
    and IRMs would indicate and provide a control rod block or scram 
    signal, as appropriate, to an increase in neutron flux to mitigate a 
    transient event. Furthermore, should the number of OPERABLE IRM or SRM 
    channels be less than that required by Technical Specifications, the 
    Technical Specifications require that core alteration activities be 
    suspended and all insertable control rods be inserted into the core.
        Therefore, the proposed Technical Specification changes do not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        III. This change does not involve a significant reduction in a 
    margin of safety.
        For the reasons discussed in items 1 and 2 above and because the 
    Technical Specification Bases do not discuss or require APRMs 
    operability during OPCON 5, Refueling, the proposed Technical 
    Specification changes do not involve a significant reduction in a 
    margin of safety.
        The NRS staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration. Local 
    Public Document Room location: Osterhout Free Library, Reference 
    Department, 71 South Franklin Street, Wilkes-Barre, Pennsylvania 18701 
    Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Philadephia Electric Company
    
    Docket Nos. 50-352 and 50-353
    
        Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania.
        Date of amendment request: August 22, 1994.
        Description of amendment request: The amendment consists of five 
    (5) sections of Technical Specifications changes which reflect the 
    Improved Standard Technical Specifications (NUREG-1433):
    
    Section 1: Control Rod Block Instrumentation,
    Section 2: Standby Liquid Control System Operability in Mode 5,
    Section 3: Scram Discharge Volume Valve Testing,
    Section 4: Optional Method of Scram Timing, and
    Section 5: Definition of Core Alteration.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    Section 1: Control Rod Block Instrumentation
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed TS changes can be divided into two general categories, 
    the deletion of the ``S/U'' requirements, and the change in frequency 
    of the SRM [Source Range Monitor] and IRM [Intermediate Range Monitor] 
    Calibration and Functional Tests. In each case in which the ``S/U'' 
    requirement has been deleted, the normal surveillance frequency 
    specified for the required Operating Condition remains. The equipment's 
    associated probability of failure remains unchanged. In the case of the 
    surveillance frequency changes proposed for the SRMs and IRMs, the 
    probability of an accident evaluated in the SAR [Safety Analysis 
    Report] occurring does not increase since there is no credit taken in 
    the SAR for those Control Rod Block functions with respect to an 
    accident. As such, the proposed changes will not result in an increase 
    in the probability of occurrence of an accident previously evaluated in 
    the SAR. The proposed TS changes do not alter the method of operation 
    or performance of the equipment in carrying out associated Control Rock 
    Block functions. Thus, the consequences of an accident previously 
    evaluated in the SAR are not increased.
        Therefore, the proposed TS changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed TS changes do not alter the configuration of the plant 
    or the way that the plant is operated. The equipment can perform no 
    other function than it is presently capable of, or cause or permit any 
    other accident than is now possible. Thus, the possibility of an 
    accident of a different type than previously evaluated in the SAR 
    cannot be created.
        Therefore, the proposed TS changes do not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. The proposed TS changes do not involve a significant reduction 
    in a margin of safety.
        Since the proposed TS changes affect only the surveillance 
    frequency intervals and do not change the plant configuration or 
    associated instrument setpoints, there is no quantitative or 
    qualitative reduction in the margin of safety. Thus, the margin of 
    safety as defined in the bases of any Technical Specification is not 
    reduced.
        Therefore, the proposed TS changes do not involve a reduction in a 
    margin of safety.
    Section 2: Standby Liquid Control System Operability in Mode 5
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed TS change will remove the SLCS operability requirement 
    in OPCON 5. The purpose of the SLCS is to bring the reactor to and 
    maintain it in a cold shutdown condition from normal power operations 
    following failure to scram during power operations. Initiation of the 
    SLCS is not a precursor to any accident. Therefore, inoperability of 
    the SLCS in OPCON 5 cannot increase the probability of an accident 
    previously evaluated.
        The proposed TS change does not involve a physical change in any 
    system's configuration and no new modes of operation are introduced. 
    The SLCS has not analyzed function OPCON 5. The probability of fuel 
    failure will not be increased by this change. Shutdown margin, in 
    conjunction with TS requirements and procedural controls, will assure 
    that an inadvertent criticality event will not occur during refueling. 
    In addition, the Reactor Protection System (RPS) and Control Rod System 
    will provide protection in the unlikely event that an inadvertent 
    criticality should occur.
        Therefore, the proposed TS change does not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed TS changes does not involve a physical change in any 
    system's configuration and no new modes of operation are introduced. 
    The SLCS's only purpose is to mitigate the consequences of a failure to 
    scram during power operation. In OPCON 5, the SLCS has no analyzed 
    function, therefore, the proposed TS change will not create the 
    possibility of a new or different kind of accident from any previously 
    evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        The purpose of the SLCS is to bring the reactor to and maintain it 
    in a cold shutdown condition from normal power operations following a 
    failure to scram during power operations. The SLCS is not designed to 
    terminate an inadvertent criticality during OPCON 5. Shutdown margin, 
    either demonstrated or analytically determined, in conjunction with 
    Technical Specifications and procedural controls, will assure that an 
    inadvertent criticality event will not occur during refueling 
    operations. In addition, the RPS and Control Rod System, which are 
    extremely reliable, will provide protection in the unlikely event that 
    an inadvertent criticality does occur. Therefore, the proposed TS 
    change does not involve a reduction in a margin of safety.
    Section 3: Scram Discharge Volume Valve Testing
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The Scram Discharge Volume (SDV) is not an accident initiator. 
    Deletion of the requirement that the SDV be determined OPERABLE by 
    testing the SDV vent and drain valves when control rods are scram 
    tested from a normal control and configuration of less than or equal to 
    50% rod density at least once per 24 months, as proposed, will have no 
    effect on the probability or consequences of an accident previously 
    evaluated.
        This proposed TS will have a negligible impact on the conditions 
    experienced by the vent and drain valves as they stroke closed, since 
    the SDV is initially vented to the atmosphere, and the valves close 
    before the SDV becomes pressurized, even during a scram at full reactor 
    power. Reactor pressure and Control Rod Drive (CRD) discharge flow 
    conditions do not influence the SDV vent and drain closure rates, since 
    the SDV is of sufficient volume and initially vented such that peak 
    pressure prior to the SDV complete isolation will not be substantial. 
    In addition, lower coolant temperatures expected during testing at 
    shutdown conditions will also have a negligible impact on the 
    performance of the test. Although, there could be some variation in the 
    performance [of] the SDV vent and drain valves to re-open when 
    performing the test during shutdown conditions, as opposed to 
    conducting the test during power operation, the ability of the valves 
    to re-open is demonstrated after each reactor scram during power 
    operation.
        In the event and SDV vent or drain valve failed to open, increasing 
    SDV level during reactor operation would cause 1) an alarm in the Main 
    Control Room (MCR), 2) a control rod block, and finally a reactor scram 
    initiated by the Reactor Protection System (RPS) if action is not taken 
    to drain the SDV. Therefore, the ability to shut down the reactor is 
    not impaired. If a SDV vent or drain valve fails to close, the 
    redundant valve's closure would provide the required function. If both 
    valves failed to close, a loss of reactor coolant in the form of water 
    discharged from the CRD system would occur. The amount of water 
    discharged will be relatively small, and is more of a concern from the 
    standpoint of contamination to the Secondary Containment rather than a 
    loss of reactor water inventory. A structural failure of the SDV, which 
    bounds this case of an open SDV vent or drain line, has been previously 
    evaluated in NUREG-0808, ``Generic Safety Evaluation Report Regarding 
    Integrity of BWR Scram System Piping.'' In this evaluation, the NRC 
    concluded that, for a bounding leakage case corresponding to a rupture 
    of the SDV, the offsite doses would be well within the limits of 
    10CF100, and that adequate core cooling would be maintained.
        Deletion of the requirement that the SDV be determined OPERABLE by 
    testing the SDV vent and drain valves, as proposed in this TS Change 
    Request, will have an insignificant effect on the probability of 
    occurrence of malfunction of any plant equipment. The conditions in the 
    SDV at the time of vent and drain valve closure are not appreciably 
    different whether a scram is initiated from power operation or during 
    shutdown conditions. In addition, this proposed TS change eliminates 
    the potential need for an additional startup and shutdown cycle, along 
    with the associated challenges to all systems and components, that 
    would be required to satisfy the current TS requirements in the event a 
    unit were to trip off-line shortly before a planned outage when the 
    surveillance was scheduled to be performed. Furthermore, this proposed 
    TS changes does not affect the testing frequency for the valves.
        This proposed TS change will not result in appreciably different 
    conditions experienced by the valves as they close, and their ability 
    to re-open is confirmed following each reactor scram from power 
    conditions. The consequences resulting from a failed closed or failed 
    open SDV vent or drain line have been evaluated and determined not to 
    result in offsite doses that would exceed the limits specified in 
    10CFR100, or jeopardize adequate reactor core cooling capability. 
    Therefore, the consequences of a malfunction of equipment important to 
    safety previously evaluated is not increased.
        Therefore, the proposed TS change does not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The SDV is not an accident initiator. Deletion of the requirement 
    that the SDV be determined OPERABLE by testing the SDV vent and drain 
    valves from a configuration of less than or equal to 50% rod density, 
    as proposed, will not create the possibility of a different type [of] 
    accident than any previously evaluated.
        No plant equipment is added or deleted as a result of this proposed 
    change. Since the initial conditions of pressure, temperature, and CRD 
    system discharge flowrate have no appreciable effect on the SDV vent 
    and drain valve performance, no different type of malfunction of any 
    equipment important to safety is created.
        Therefore, the proposed TS change does not create the possibility 
    of a new different kind of accident from any previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        Since the initial test conditions of pressure, temperature, and CRD 
    discharge flowrate will have no appreciable effect on the SDV vent and 
    drain valve performance, conducting the surveillance test during 
    shutdown conditions, as specified in this proposed TS change, will not 
    affect the validity of the surveillance results with respect to the 
    operability of the SDV to perform its intended safety function. 
    Furthermore, every reactor scram is a serious plant transient and a 
    potential challenge to safety-related systems and equipment. The 
    potential decrease in future scrams which could result from this 
    proposed TS change will represent an improvement in overall safety.
        Therefore, the proposed TS change does not involve a reduction in a 
    margin of safety.
    Section 4: Optional Method of Scram Timing
        1. The proposed Technical Specification (TS) changes involves a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        Scram testing control rods at zero reactor coolant pressure will 
    not increase the probability of any control rod related transient or 
    accident discussed in the UFSAR [Updated Final Safety Analysis Report]. 
    UFSAR Sections 15.4.1.1 and 15.4.1.2 discuss the consequences of 
    inadvertent reactivity insertion errors due to the withdrawal of one or 
    more control rods. The probability of one of these events occurring is 
    a function of operator error and equipment malfunction and is not 
    related to scram insertion times.
        An inadvertent reactivity insertion error is prevented by existing 
    system hardware interlocks and procedural controls that are not 
    affected by scram time testing, e.g., core design, control and design, 
    one-rod-out interlocks, refueling interlocks, control rod sequence 
    designations, and neutron monitoring systems.
        USFAR Section 15.4.9 discusses the control rod drop accident 
    (CRDA). The CRDA assumes that a control rod suddenly drops out of the 
    core due to equipment malfunction. The probability of occurrence of 
    this accident is based on an equipment malfunction and is not affected 
    by scram testing.
        Engineering analysis and control rod scram test data demonstrate 
    that a control rod drive that will meet the 2.0 second, scram insertion 
    time, test criteria at zero reactor coolant pressure will also meet all 
    scram insertion criteria during reactor startup and up to 40% rated 
    thermal power.
        The 2.0 second criterion was chosen to conservatively envelop scram 
    time criteria and reactivity insertion criteria during reactor startup 
    and up to 40% rated power conditions. Therefore, scram testing affected 
    control rods at zero reactor pressure will not increase the 
    consequences of an accident previously evaluated.
        UFSAR Sections 15.4.1.1 and 15.4.1.2 evaluate reactivity insertion 
    transients at low power conditions due to inadvertent control rod 
    withdrawal errors. The UFSAR concludes that rod withdrawal errors at 
    low power are adequately precluded by refueling interlocks, rod worth 
    minimizer, operating procedures, core design, and control rod hardware 
    design. However, should operator errors followed by equipment 
    malfunctions result in an inadvertent criticality event, the IRMs would 
    provide the necessary rod blocks or reactor scram to preclude the 
    operational transient. Scram insertion time limits for the continuous 
    rod withdrawal error during startup is 5.0 seconds. This scram time 
    criterion will be met by a control rod that scrams within 2.0 seconds 
    at zero reactor pressure. The 2.0 second scram criterion was 
    established to ensure that affected control rods will meet scram 
    requirements from zero reactor pressure up to 40% core thermal power.
        Also, during low power operation (UFSAR Subsection 15.4.1.2) the 
    rod worth minimizer (RWM) prevents the operator from selecting and 
    withdrawing an out-of-sequence control rod. During reactor operation in 
    the power range (UFSAR subsection 15.4.2) the rod block monitor (RBM) 
    prevents a rod withdrawal error by inhibiting inadvertent control rod 
    withdrawal. The RWM and RBM do not rely on a scram function to 
    mitigation the consequences of a rod withdrawal error, and therefore 
    the consequences of an accident evaluated in the UFSAR will not be 
    affected by the proposed changes to the Technical Specifications.
        The consequences of a control rod drop accident (UFSAR Section 
    15.4.9) would not be affected by scram testing a control rod at zero 
    reactor pressure. The design basis accident of the rod drop accident 
    assumes that control rods scram within 5.0 seconds. This 5.0 second 
    scram test requirement will be met by control rods that meet the 2.0 
    second criterion at zero reactor pressure.
        Therefore, the proposed TS changes do not involve an increase in he 
    probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The changes to the Technical Specifications will allow control rods 
    to be scram tested at zero reactor pressure and then again at rated 
    reactor pressure prior to achieving 40% rated reactor power. No new 
    types of accidents will be introduced since control rods that meet the 
    2.0 second scram criterion at zero reactor pressure will also meet all 
    scram test criteria during reactor startup and at rated reactor 
    pressure.
        Therefore, the proposed TS changes do not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. The proposed TS changes do not involve a significant reduction 
    in a margin of safety.
        The basis for shutdown margin (TS Bases 3/4.1.1) states that the 
    reactor shall be made subcritical by all certain margin in all 
    operating and shutdown conditions. The proposed changes to the 
    Technical Specifications will not affect the shutdown margin 
    requirements. Adequate shutdown margin is assured by core design, the 
    one-rod-out interlock, and administrative controls.
        The basis for the control rod insertion times (TS Bases 3/4.1.3) 
    states that the scram times are to be consistent with those used in the 
    transient and accident analysis. The proposed Technical Specifications 
    changes will add an additional scram test verification for affected 
    control rods at zero reactor pressure. The zero reactor pressure scram 
    limit (2.0 seconds) was designed to ensure that the scram times assumed 
    in the transient analysis will remain bounding from zero reactor 
    pressure up to 40% rated core thermal power.
        The basis for the control rod drop accident (TS Bases 3/4.1.3) 
    states that the potential effects of a CRDA are limited. The proposed 
    Technical Specifications changes will not effect the control rod drop 
    results as the changes do not affect the reactivity of the rod or the 
    rod drop velocity. The CRDA analysis is based on a 5.0 second scram 
    insertion time criterion. The 2.0 second time criterion was established 
    to ensure that the 5.0 second scram time criterion was valid from zero 
    reactor pressure to 950 psig reactor pressure.
        The basis for MCPR limits (TS Bases 3/4.1.3 and 2.3) states the CRD 
    system must bring the reactor subsubcritical at a rate fast enough to 
    prevent MCPR from becoming less than the fuel cladding safety limit 
    during the limiting power transient analyzed in the UFSAR. The proposed 
    changes to the Technical Specifications will not affect the scram 
    insertion rates that are used as input to the transient analysis. The 
    zero reactor pressure scram limit of 2.0 seconds was developed to 
    ensure that the control rods would meet their design scram insertion 
    times from zero reactor pressure up to 40% rated power.
        The proposed changes to the Technical Specifications will not 
    increase the probability of inadvertent criticality because the changes 
    do not affect the reactivity worth of control rods.
        Therefore, the proposed TS changes do not involve a reduction in a 
    margin of safety.
    Section 5: Definition of Core Alteration
        1. The proposed TS change does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        The proposed definition change removes the requirement to have a 
    SRO or LSRO supervise control rod withdrawal in an off-loaded cell 
    (i.e. no fuel assemblies). The evaluated accident potentially affected 
    by this change is a control rod movement error during refueling 
    resulting in inadvertent criticality. The supervision by a SRO or LSRO 
    does not solely preclude inadvertent criticality and was not relied 
    upon in the accident analysis contained in Section 15.4 of the LGS 
    Updated Final Safety Analysis Report (UFSAR). The LGS reactor core is 
    designed to have adequate shutdown margin with the highest-reactivity-
    worth control rod withdrawn. The withdrawal of a second rod with fuel 
    assemblies loaded in the associated cell is prevented by a combination 
    of the refueling, one-rod-out interlock, and the Limiting Conditions 
    for Operation (LCO) requirement of TS 3.9.10.2. The LCO requirements 
    ensure adequate shutdown margin is present prior to control rod 
    withdrawal. This is accomplished by testing during startup following a 
    refueling outage or by analytical calculations during refueling. The 
    refueling interlock will provide a rod block upon an attempt to 
    withdraw a second control rod and is required to be operable in 
    accordance with TS 3.9.10.2 except for rods which have no fuel 
    assemblies in the associated cell. The removal of the fuel assemblies 
    from a cell eliminates the need for the reactivity control function of 
    the associated rod. The physical removal of a control blade from the 
    core by means of the refueling floor, first requires the removal of the 
    four associated fuel assemblies in the cell. This design inherently 
    prevents inadvertent criticality. Finally, this change is consistent 
    with NUREG-1433 ``Standard Technical Specifications.'' Since current 
    analysis permits the withdrawal of a control rod blade, provided the 
    associated cell is unloaded, and refueling mode interlocks, 
    administrative TS requirements and the physical design of the control 
    blade and fuel cell, which preclude inadvertent criticality, will 
    remain unchanged, this proposed change to the TS definition of CORE 
    ALTERATION will not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The LGS UFSAR currently permits control rod withdrawal and or 
    removal, provided there are no fuel assemblies in the associated fuel 
    cell. The definition change removes the requirement to have a SRO or 
    LSRO supervise rod withdrawal in an off-loaded cell. The change 
    potentially [a]ffects a control rod movement error during refueling 
    resulting in inadvertent criticality which has been previously 
    evaluated. In addition, the proposed change will make no physical 
    changes to equipment or remove administrative controls which solely 
    preclude inadvertent criticality. Therefore, this change will not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        The LGS TS bases address reactivity concerns, radiological 
    releases, control rods, and monitoring of the facility related to this 
    change. With the four fuel assemblies removed from a cell, the control 
    rod/blade in the associated cell has no reactivity function. The 
    reactivity issues addressed by TS are therefore unaffected. The rod/
    blade coupling integrity is maintained by the requirement to perform a 
    coupling check following maintenance. Section 15.4 of the UFSAR states 
    that there are no radiological releases in association with a rod 
    withdrawal error during refueling. This conclusion is maintained by the 
    administrative requirements of TS 3.9.10.2, the refueling interlocks 
    for one-rod-out, and the physical design of the blade and cell. Lastly, 
    the TS requirements for Emergency Core Cooling, Plant System, 
    Containment, and Electrical Power Distribution System, which provide 
    the systems necessary to mitigate the effects of a radiological release 
    during control rod movement in an unloaded cell were reviewed and were 
    found not to be adversely [a]ffected by the proposed change. Therefore, 
    this change will not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J.W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: John F. Stolz.
    
    Philadelphia Electric Company
    
    Docket Nos. 50-352 and 50-353
    
        Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania.
        Date of amendment request: August 31, 1994.
        Description of amendment request: The proposed amendments, which 
    are consistent with the Improved Standard Technical Specifications 
    (NUREG-1433), involve the following six (6) sections of TS changes:
    
    Section 1: Relocation of Turbine Overspeed Protection System 
    Requirements;
    Section 2: Relocation of Primary Containment Conductor Protection 
    Devices Requirements;
    Section 3: Feedwater/Main Turbine Trip System Actuation Instrumentation 
    Requirements;
    Section 4: Permit Operability of Low Pressure Coolant Injection While 
    Aligned to Shutdown Cooling;
    Section 5: Remove Temperature Requirement for Operational Condition 
    [OPCON] 5; and
    Section 6: Reduce Frequency of Alternate Decay Heat Demonstration
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    Section 1: Relocation of Turbine Overspeed Protection System 
    Requirements
        1. The proposed TS change does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        The proposed change relocates requirements from the TS, to licensee 
    controlled documents. The licensee controlled documents containing the 
    relocated requirements will be maintained using the provisions of 10 
    CFR 50.59 and are subject to the change control process in the 
    Administrative Controls Section 6.0 of the TS. Since changes to 
    licensee controlled documents will be evaluated per 10 CFR 50.59, no 
    increase (significant or insignificant) in the probability or 
    consequences of an accident previously evaluated will be allowed. 
    Therefore, this change will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident previously evaluated.
        This change relocates requirements to licensee controlled 
    documents. This change will not alter the plant configuration (no new 
    or different type of equipment will be installed) or make changes in 
    methods governing normal plant operation. This change will not impose 
    different requirements and adequate control of information will be 
    maintained. This change will not alter assumptions made in the safety 
    analysis and licensing basis. Therefore, this change will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        This change relocates requirements from the TS to licensee 
    controlled documents. This change will not reduce a margin of safety 
    since it has no impact on any safety analysis assumptions. In addition, 
    the requirements to be transferred from the TS to licensee controlled 
    documents are the same as the existing Technical Specifications. Since 
    any future changes to these licensee controlled documents will be 
    evaluated per the requirements of 10 CFR 50.59, no reduction 
    (significant or insignificant) in [a] margin of safety will be allowed. 
    Therefore, this change will not involve a significant reduction in a 
    margin of safety.
        The existing requirements for NRC review and approval of revisions, 
    in accordance with 10 CFR 50.59, to these details and requirements 
    proposed for relocation, does not have a specific margin of safety upon 
    which to evaluate. However, since the proposed change is inconsistent 
    with the BWR [boiling-water reactor] Improved Standard Technical 
    Specifications (NUREG-1433 approved by the NRC Staff) and the change 
    controls for proposed relocated details and requirements provide an 
    equivalent level of regulatory authority, revising the TS to reflect 
    the approved level of detail and requirements ensures no reduction to 
    the margin of safety.
    Section 2: Relocation of Primary Containment Conductor Protection 
    Devices Requirements
        1. The proposed TS change does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        This proposed change relocates requirements from the TS to licensee 
    controlled documents. The licensee controlled documents containing the 
    relocated requirements will be maintained using the provisions of 10 
    CFR 50.59 and are subject to the change control process in the 
    Administrative Controls Section 6.0 of the TS. Since changes to these 
    licensee controlled documents will be evaluated per 10 CFR 50.59, no 
    increase (significant or insignificant) in the probability or 
    consequences of an accident previously evaluated will be allowed. 
    Therefore, this change will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        This change relocates requirements to licensee controlled 
    documents. This change will not alter the plant configuration (no new 
    or different type of equipment will be installed) or make changes in 
    methods governing plant operation. This change will not impose 
    different requirements and adequate control of information will be 
    maintained. This change will not alter assumptions made in the safety 
    analysis and licensing basis. Therefore, this change will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        This change relocates requirements from the TS to licensee 
    controlled documents. This change will not reduce a margin of safety 
    since it has no impact on any safety analysis assumptions. In addition, 
    the requirements to be transferred from the TS to the licensee 
    controlled documents are the same as the existing TS. Since any future 
    changes to these licensee controlled documents will be evaluated per 
    the requirements of 10 CFR 50.59, no reduction (significant or 
    insignificant) in [a] margin of safety will be allowed. Therefore, this 
    change will not involve a significant reduction in a margin of safety.
        The existing requirements for NRC review and approval of revisions, 
    in accordance with 10 CFR 50.59, to these details and requirements 
    proposed for relocation, does not have a specific margin of safety upon 
    which to evaluate. However, since the proposed change is consistent 
    with the BWR Improved Standard TS (NUREG-1433 approved by the NRC 
    Staff) and the change controls for proposed relocated details and 
    requirements provide an equivalent level of regulatory authority, 
    revising the TS to reflect the approved level of detail and 
    requirements ensures no reduction to the margin of safety.
    Section 3: Feedwater/Main Turbine Trip System Actuation Instrumentation 
    Requirements
        1. The proposed TS change does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        For the proposed TS change, in the event of a Reactor Vessel Water 
    Level--High Level 8 transient, operator action per existing plant 
    procedures would terminate the event and prevent damage to the Main/RFP 
    [reactor feed pump] Turbine due to water carry over. The Main/RFP 
    Turbine do not serve a safety function, also at <25% [rated="" thermal="" power]="" rtp="" a="" level="" 8="" transient="" event="" will="" not="" cause="" a="" reactor="" scram.="" an="" analysis="" of="" information="" in="" the="" bases="" for="" aplhgr="" [average="" planar="" linear="" heat="" generation="" rate]="" and="" mcpr="" [minimum="" critical="" power="" ratio]="" has="" shown="" that="" a="" sufficient="" margin="" to="" core="" safety="" limit="" exist,="" so="" fuel="" integrity="" levels="" are="" not="" violated.="" therefore,="" the="" proposed="" ts="" change="" does="" not="" involve="" an="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" 2.="" the="" proposed="" ts="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" should="" the="" feedwater/main="" turbine="" trip="" system,="" reactor="" vessel="" water="" level-high="" level="" 8,="" not="" actuate="" in="" opcon="" 1="" at=""><25% rtp,="" operator="" action="" per="" existing="" plant="" startup="" procedures="" would="" protect="" the="" main/rfp="" turbines.="" if="" operator="" action="" is="" not="" performed,="" damage="" to="" balance="" of="" plant,="" non-safety="" related="" equipment="" could="" occur.="" high="" reactor="" vessel="" water="" level="" is="" not="" a="" concern="" for="" reactor="" core="" safety="" at=""><25% rtp.="" therefore,="" the="" proposed="" ts="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" 3.="" the="" proposed="" ts="" change="" does="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" proposed="" ts="" change,="" which="" revises="" the="" feedwater/main="" turbine="" trip="" system="" actuation="" instrumentation,="" reactor="" vessel="" water="" level-high="" level="" 8,="" operability="" requirements,="" does="" not="" affect="" the="" ts="" bases.="" the="" trips="" are="" designed="" to="" protect="" balance="" of="" plant="" equipment="" at="" all="" rate="" power="" levels.="" the="" reactor="" vessel="" water="" level-high="" level="" 8="" trips="" also="" protects="" fuel="" integrity="" at="">25% RTP. Therefore, the proposed TS change 
    to the operability requirements for the feedwater/main turbine trip 
    system actuation instrumentation does not involve a reduction in a 
    margin of safety.
    Section 4: Permit Operability of Low Pressure Coolant Injection While 
    Aligned to Shutdown Cooling
        1. The proposed Technical Specifications change does not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        The LPCI [low pressure coolant injection] mode of RHR is an 
    accident mitigator, not an initiator. Currently, the LPCI mode of RHR 
    is an automatic Emergency Core Cooling System (ECCS) function during 
    OPCONs 4 and 5. However, shutdown cooling has been an accident 
    initiator in many industry events. Reliance on this loop of RHR for 
    LPCI does not increase the probability of an accident in shutdown 
    cooling, but the alignment for LPCI will, in itself, terminate the 
    draindown event by exiting the shutdown cooling mode. This proposed 
    change will permit the operability of one LPCI subsystem while the 
    components of that subsystem are aligned and operating in the Shutdown 
    Cooling mode of RHR, provided all other components of that subsystem 
    are operable and can be manually realigned from the Main Control Room, 
    if required. The required number of operable Emergency Core Cooling 
    Systems (ECCS) remains unchanged, thus maintaining the TS required 
    subsystem redundancy (TS Section 3.5.2 requires two operable ECCS 
    subsystems with exception for Reactor level). With this change, the 
    required number of LPCI subsystems are capable of performing their 
    function of limiting and/or mitigating the consequences of an accident, 
    by allowing the manual alignment of one LPCI subsystem, during OPCONs 4 
    and 5. This allowance is justified since the change only applies to 
    OPCONs 4 and 5, when reactor temperature, and associated heat loads are 
    sufficiently low to provide the operator sufficient time to perform the 
    manual realignment, from the Main Control Room, of the RHR pump suction 
    valves and restart of the pump following LPCI injection conditions. 
    Similar allowances for LPCI are currently permitted during OPCON 3, 
    since the decay heat loads are significantly reduced compared to OPCON 
    1, which is the mode of operation under which ECCS capability is 
    analyzed (Section 6.3 of the LGS [Limerick Generating Station] Updated 
    Final Safety Analysis Report (UFSAR)). The change will not increase the 
    probability of occurrence or consequences of a malfunction of equipment 
    since there will be no physical changes made to plant equipment nor the 
    method of their operation that would result in an unanalyzed condition. 
    PECO Energy [Philadelphia Electric Company] evaluated the need for 
    manual realignment of the pump minimum flow path since operating in 
    Shutdown Cooling typically results in the isolation of the pump minimum 
    flow path to prevent inadvertent draining of the reactor vessel. The 
    associated pump is still operable since this change is limited to 
    OPCONs 4 and 5, when reactor pressure is sufficiently low to allow 
    immediate injection to the reactor vessel without a minimum flow path. 
    In situations, while in OPCON 4, where reactor pressure may not be 
    sufficiently low to allow injection, the RHR system will not be aligned 
    for Shutdown Cooling, since the reactor vessel pressure will be greater 
    than the RHR ``cut-in'' permissive pressure. In addition, 
    Administrative Controls are currently in place to realign RHR to the 
    LPCI mode for planned pressure increases. Finally, this change is 
    consistent with NUREG-1433 ``Standard Technical Specifications.'' 
    Therefore, these changes will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The LPCI mode of RHR is an accident mitigator, not an initiator. 
    This change will not reduce the number of required ECCS during OPCONs 4 
    and 5. This change will permit the operability of one LPCI subsystem 
    while the components of that subsystem are aligned and operating in the 
    Shutdown Cooling mode of RHR. The change does not alter current methods 
    of plant operation nor does the change make a physical change to plant 
    equipment resulting in an unanalyzed malfunction of equipment. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        The basis of TS Section 3.5.2 is to ensure sufficient ECCS capacity 
    to maintain core cooling in OPCONs 4 and 5. This proposed change does 
    not affect the required number of ECCS during OPCONs 4 and 5; 
    therefore, adequate capability through subsystem redundancy is 
    maintained. The amount of time required to obtain rated LPCI conditions 
    is increased due to the manual realignment, from the Main Control Room, 
    of the suction valves and restart of the RHR pump following LPCI 
    injection conditions. This change is in conformance with the current TS 
    bases, since the operator has sufficient time to perform the manual 
    realignment, during OPCONs 4 and 5, ensuring sufficient ECCS capability 
    to maintain core coverage. In addition, NUREG-1433 BASES states, in 
    part, ``One LPCI subsystem may be aligned for decay heat removal and 
    considered OPERABLE for the ECCS function, if it can be manually 
    realigned (remote or local) to the LPCI mode and is not otherwise 
    inoperable. Because of low pressure and low temperature conditions in 
    MODES 4 and 5, sufficient time will be available to manually align and 
    initiate LPCI subsystem operation to provide core cooling prior to 
    postulated fuel uncover.'' Therefore, this change will not involve a 
    significant reduction in a margin of safety.
    Section 5: Remove Temperature Requirement for Operational Condition 5
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed TS change does not involve a physical change in the 
    configuration of any systems important to safety. The elimination of a 
    temperature requirement from the definition of OPCON 5 was reviewed for 
    potential effect on reactor coolant system materials and for potential 
    effect on reactivity. This TS change does not result in system 
    temperature and pressure change or reactivity changes not previously 
    analyzed. The reactor pressure vessel will still be restricted to the 
    temperature and pressure limits of TS Section 3/4.4.6 which includes 
    heatup/cooldown rates and minimum boltup limits. The reactor pressure 
    vessel temperature and pressure limits will still ensure proper 
    protection of the reactor coolant system materials. Therefore, this TS 
    change does not increase the probability or consequences of an accident 
    previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed TS change does not involve any physical change in 
    plant configuration, and reactor coolant system temperature and 
    pressure are still restricted per TS Selection 3/4.4.6. The decrease in 
    moderator density corresponding to the potential change in temperature 
    (i.e., above 140 deg.F and below 200 deg.F) would have a negligible, 
    however conservative effect on shutdown margin. Therefore, this TS 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        This proposed TS change does not change the reactor coolant system 
    material restrictions as defined in TS Section 3/4.4.6. Therefore, the 
    reactor pressure vessel will still be maintained under the current 
    temperature and pressure restrictions as well as the current boltup 
    limits.
        The decrease in moderator density corresponding to the potential 
    temperature change from 140 deg.F to 200 deg.F is insignificant and 
    would afford approximately the same moderator effect. Therefore, 
    shutdown margin could only be improved (although marginally) at these 
    evaluated temperatures. The actual coolant temperature will be 
    administratively controlled to provide for personnel safety. Therefore, 
    this change will not involve a reduction in a margin of safety.
    Section 6: Reduce Frequency of Alternate Decay Heat Demonstration
        1. The proposed TS change does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        The proposed TS change does not involve any physical changes to 
    plant systems or equipment. This proposed TS change will allow the use 
    of either an ``analytical approach'' (i.e., calculation) or 
    ``demonstration'' to ensure the operability of an alternate decay heat 
    removal method. This proposed TS change does not involve any physical 
    changes to plant systems or components, nor does it affect the 
    capability, availability, or operability of any decay heat removal 
    systems/methods (e.g., Shutdown Cooling). The Shutdown Cooling mode of 
    operation of the Residual Heat Removal (RHR) system, and Residual Heat 
    Removal Service Water (RHRSW) system, are not impacted by this proposed 
    TS change, and will continue to function as designed to remove decay 
    heat loads from the reactor primary coolant system. The RHRSW system 
    and various modes of operation of the RHR system, e.g., Low Pressure 
    Coolant Injection (LPCI) are not accident initiators, since these 
    systems function to mitigate the consequences of an accident. This 
    proposed TS change is consistent with the criteria delineated in the 
    Improved Standard TS (i.e., NUREG-1433, ``Standard Technical 
    Specifications, General Electric Plants, BWR/4,'' dated September 28, 
    1992).
        Therefore, the proposed TS change does not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        This proposed TS change does not involve any physical changes to 
    plant systems or equipment. The proposed TS change will allow the use 
    of a ``calculation'' or ``demonstration'' as the means for determining 
    the operability of an alternate decay heat removal method. The proposed 
    TS change does not involve any physical changes to plant systems or 
    equipment. This proposed TS change will not affect the operation of the 
    Shutdown Cooling mode of the RHR system. This mode of operation will 
    continue to function as designed to remove decay heat loads from the 
    reactor primary coolant system. This proposed TS change will not impact 
    the operation of the other modes of operation of the RHR system (e.g., 
    LPCI), nor will it affect the operation of the RHRSW system. These 
    systems will continue to function as designed, which is to mitigate the 
    consequences of an accident. This proposed TS change will not introduce 
    the potential for equipment malfunctions or failures. This proposed TS 
    change is consistent with the criteria delineated in the Improved 
    Standard TS (i.e., NUREG-1433).
        Therefore, the proposed TS change does not create the possibility 
    of a new or different kind of accident from any previously evaluated.
        3. The proposed TS change does not involve a significant reduction 
    in a margin of safety.
        The proposed change to the TS does not involve any physical changes 
    to plant systems or equipment. This proposed TS change does not make 
    any physical modifications to plant systems or equipment, and is 
    consistent with the criteria delineated in the Improved Standard TS 
    (i.e., NUREG-1433). The proposed TS change will not impact any mode of 
    operation of the RHR system or the RHRSW system.
        This proposed TS change involves revising TS ACTION statements, and 
    associated supporting Bases sections, to allow for the use of a 
    ``calculation'' or ``demonstration'' to ensure the operability of an 
    alternate decay heat removal method. The bases for the TS sections 
    affected by this proposed change indicate that sufficient heat removal 
    capability, system redundancy, and coolant circulation will be 
    available to facilitate decay heat removal and mixing to assure 
    accurate temperature indication.
        This proposed TS change does not affect the function or 
    availability of any decay heat removal system or method.
        Therefore, the proposed TS change does not involve a reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J.W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: John F. Stolz.
    
    Power Authority of the State of New York
    
    Docket No. 50-333
    
        James A. FitzPatrick Nuclear Power Plant, Oswego County, New York.
        Date of amendment request: October 3, 1994.
        Description of amendment request: The proposed amendment would 
    extend the functional test intervals and allowable out-of-service times 
    for some of the instruments subject to requirements of the Technical 
    Specifications (TSs). These proposed changes are based upon NRC-
    approved Licensing Topical Reports prepared under the direction of the 
    Boiling Water Reactors Owners Group and intended to enhance plant 
    safety by reducing the potential for test related scrams, excessive 
    test cycles on equipment, and operator errors. The proposed amendment 
    would also: (1) Remove the Average Power Range Monitor (APRM) downscale 
    scram function from the TSs, remove instrument response time values 
    from the TSs in accordance with Generic Letter 93-08, and incorporate 
    various editorial changes and clarifications into the TSs. The proposed 
    amendment involves reactor protection system, primary containment 
    isolation, emergency core cooling, control rod block, and anticipated 
    transient without scram recirculation pump trip instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the proposed 
    Amendment would not involve a significant hazards consideration as 
    defined in 10 CFR 50.92, since it would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
    
    a. Incorporate STI [Surveillance Test Interval] and AOT [Allowable Out-
    Of-Service Time] Improvement--Category 1
    
        The proposed changes are limited to an extension of the 
    surveillance testing intervals and allowable out-of-service times of 
    plant instrumentation. The changes do not introduce any new modes of 
    plant operation, make any physical changes, or alter any operational 
    setpoints. Therefore, the changes do not degrade the performance of any 
    safety system assumed to function in the accident analysis. 
    Consequently, there is no effect on the probability of occurrence of an 
    accident.
        Regarding the consequences of an accident, the GE [General Electric 
    Company] Licensing Topical Reports (References 1 through 7) concluded 
    that the proposed extensions in the STI and AOT for the safety system 
    instrumentation results in an insignificant change in the core damage 
    frequency. The extension of the STI/AOTs results in a slight increase 
    in the unavailability of the safety functions. However, this effect is 
    offset by a reduction in the probability of inadvertent plant trips due 
    to reduced testing. The overall effect on the probability of an 
    accident is negligible. While the effects of reducing unnecessary 
    cycles on safety system instrumentation is not quantifiable, the effect 
    will be to further reduce the core damage frequency. The NRC concurred 
    in their SERs [Safety Evaluation Reports] (References 8 through 15) 
    with these conclusions. Consequently, there is not a significant 
    increase in the consequences of an accident.
    
    b. Relocation of the Instrument Response Time Limits--Category 2
    
        The change involves the use of an alternate regulatory process for 
    controlling the instrument response time limits. The change does not 
    introduce any new modes of plant operation, make any physical changes, 
    alter any operational setpoints, or change the surveillance 
    requirements.
    
    c. Delete APRM Downscale Scram--Category 3
    
        The design basis accident applicable to the startup power region is 
    the Control Rod Drop Accident (CRDA). The FSAR [Final Safety Analysis 
    Report] does not credit the APRM downscale scram in the termination of 
    this accident. Accident mitigation is provided by the APRM fixed high 
    neutron flux scram. Therefore, elimination of this scram functions has 
    no adverse affect on previously evaluated accidents.
    
    d. Miscellaneous Changes--Category 4
    
        The changes do not introduce any new modes of plant operation, make 
    any physical changes, or alter any operational setpoints. The changes 
    involve enhancements that clarify the Technical Specification 
    requirements.
        2. Create the possibility of a new or different kind of accident 
    from those previously evaluated because:
    
    a. Incorporate STI and AOT Improvements--Category 1
    
        The proposed changes do not introduce any new accident initiators 
    or failure mechanisms since the changes do not introduce any new modes 
    of plant operation, make any physical changes, or alter any operational 
    setpoints. The changes reduce the probability of accidents initiated by 
    test-induced plant trips.
    
    b. Relocation of the Response Time Limits--Category 2
    
        The change involves the use of an alternate process for controlling 
    the instrument response time limits. The change does not introduce any 
    accident initiators since it does not involve any new modes of plant 
    operation, make any physical changes, alter any operational setpoints, 
    or change the surveillance requirements.
    
    c. Delete APRM Downscale Scram--Category 3
    
        Scram functions are intended to shutdown the reactor following 
    transients or accidents and their removal does not introduce an 
    accident initiator. The limiting accident evaluated in the FSAR for the 
    startup power region is the control rod drop accident. This accident is 
    assumed to occur irrespective of the scram functions provided to 
    terminate this accident.
    
    d. Miscellaneous Changes--Category 4
    
        The changes do not introduce any new accident initiators or failure 
    mechanisms since the changes do not alter the physical characteristics 
    of any plant system or component. The changes involve enhancements that 
    clarify the Technical Specification requirements.
        3. Involve a significant reduction in the margin of safety because:
    
    a. Incorporate STI and AOT Improvements--Category 1
    
        The proposed changes do not alter the manner in which safety 
    limits, limiting safety system settings, or limiting conditions for 
    operation are determined. The affected instrumentation setpoints 
    already account for the effects of drift and include sufficient 
    allowance for an extension in the STIs. The evaluations presented in 
    the referenced Licensing Topical Reports concluded that the overall 
    effect of the proposed changes provides a net increase in plant safety. 
    The improvement is achieved by reducing the potential for: (a) Test 
    related plant scrams (reduced challenges to plant shutdown systems and 
    improved plant availability); (b) excessive test cycles on equipment 
    (reduced wear-out potential); (c) operator errors (AOT provides 
    reasonable time for making repairs and tests); (d) scrams that occur 
    when inoperable channels are tripped because insufficient repair time 
    exists; and (e) diversion of plant personnel and resources on 
    unnecessary testing (potential safety and operational improvement).
    
    b. Relocation of the Response Time Limits--Category 2
    
        The change involves the use of an alternate regulatory process for 
    controlling the instrument response time limits. The change does not 
    introduce any new modes of plant operation, make any physical changes, 
    alter any operational setpoints, or change the surveillance 
    requirements.
    
    c. Delete APRM Downscale Scram--Category 3
    
        The only scram function that the UFSAR [Updated Final Safety 
    Analysis Report] takes credit for in the mitigation of the limiting 
    accident (control rod drop accident) is the APRM 15% power fixed high 
    neutron flux scram. This scram function, as well as the IRM 
    [Intermediate Range Monitor] high flux scram function in the startup 
    mode which could also terminate this accident, are not affected by this 
    change. Only the APRM downscale scram, for which the UFSAR takes no 
    credit in the termination of any analyzed event, is eliminated by this 
    change. The APRM downscale control rod block is not affected by this 
    change. Elimination of the APRM downscale scram will avoid the need to 
    operate the plant in a ``half scram'' condition for certain IRM/APRM 
    channel bypass combinations, therefore eliminating the potential for an 
    inadvertent plant transient. For these reasons, the change does not 
    involve a significant reduction in the safety margin.
    
    d. Miscellaneous Changes--Category 4
    
        The changes assure compliance with the Technical Specifications by 
    improving its clarity and accuracy. For these reasons the changes will 
    improve the plant's margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Ledyard B. Marsh.
    
    Power Authority of the State of New York
    
    Docket No. 50-333
    
        James A. FitzPatrick Nuclear Power Plant, Oswego County, New York.
        Date of amendment request: October 7, 1994.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 4.6.E.4 to establish that the 
    manual cycling of reactor coolant system (RCS) safety/relief valves 
    (SRVs) during plant startups is to be accomplished within 12 hours 
    after steam pressure and flow are adequate to perform the testing. TS 
    4.6.E.4 currently requires this testing to be performed within 12 hours 
    of continuous power operation at a reactor steam dome pressure of at 
    least 940 psig. This change was proposed to minimize the potential for 
    undesirable pressure transients in the RCS. The amendment would also 
    make several editorial changes to clarify the intent of TS's involving 
    SRV valve testing and performance requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the James A. FitzPatrick Nuclear Power Plant in 
    accordance with the proposed amendment would not involve a significant 
    hazards consideration as defined in 10 CFR 50.92, since it would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because the proposed 
    changes do not change the test method or conditions under which valve 
    testing may be performed and there is no affect on assumptions used for 
    previously analyzed accidents. The original operating license for 
    FitzPatrick did not specify any time limit for completing manual 
    testing of the safety/relief valves.
        2. Create the possibility of a new or different kind of accident 
    from those previously evaluated because the proposed amendment does not 
    involve any modification of plant equipment or changes in plant 
    operating conditions.
        3. Involve a significant reduction in the margin of safety because 
    the proposed amendment makes no changes to the operability of 
    performance requirements for the safety/relief valves including the ADS 
    [Automatic Depressurization System] function. Valve lift setpoints and 
    the minimum number of operable valves required are not affected.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Ledyard B. Marsh.
    
    Public Service Electric & Gas Company
    
    Docket Nos. 50-272 and 50-311
    
        Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey.
        Date of amendment request: September 9, 1994.
        Description of amendment request: The proposed amendment modifies 
    the visual inspection for snubbers in the Technical Specifications and 
    is consistent with the guidance provided in Generic Letter 90-09.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes involve no hardware changes, no changes to the 
    operation of snubbers, and does not change the ability of the snubbers 
    to perform their intended functions. Visual inspection of snubbers is a 
    separate process that complements the functional testing program. The 
    NRC has concluded that functional testing of snubbers provides a 95 
    percent confidence level and 90 to 100 percent of the snubbers will 
    operate within the specified acceptance limits. Any change in the 
    visual inspection frequency will not have any significant impact on the 
    operability of the snubbers.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed changes will not result in an unanalyzed condition. 
    Replacing the current method of determining visual surveillance 
    intervals with a new method approved by the NRC in Generic Letter 90-09 
    will not change the level of confidence in snubber operability. A new 
    procedure for determining visual inspection frequencies will not result 
    in an unreviewed failure mechanism.
        3. Will not involve a significant reduction in a margin of safety.
        The proposed changes incorporate the alternate Technical 
    Specification requirements for visual inspection of snubbers identified 
    in Generic Letter 90-09. The alternate visual inspection criteria 
    consider the size of the category of snubbers when evaluating 
    inspection intervals due to failure rates. Since the functional testing 
    requirements remain unchanged and do not reduce the operability 
    confidence levels, there is no resultant change in any margins of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502.
        NRC Project Director: John F. Stolz.
    
    Public Service Electric & Gas Company
    
    Docket Nos. 50-272 and 50-311
    
        Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey.
        Date of amendment request: September 20, 1994
        Description of amendment request: The proposed amendment modifies 
    the Technical Specifications for auxiliary feedwater to reduce the 
    secondary side steam pressure required for testing the steam turbine 
    driven auxiliary feedwater pump (AFW). The proposed amendment also 
    clarifies the time required to perform the steam turbine driven 
    auxiliary feedwater pump surveillance test when entering Mode 3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed change to the minimum required test pressure for the 
    steam turbine driven AFW pump does not affect the operation of the pump 
    during conditions when it is required to performed its safety function. 
    The clarification that the secondary side steam pressure is steam 
    generator pressure is editorial. Reduced Tavg and increased steam 
    generator tube plugging will affect the normal operating secondary side 
    steam pressure.
        However, the zero load secondary side steam pressure is not 
    affected, therefore, the conditions in which the steam turbine driven 
    AFW pump will be required to perform its safety function are not 
    changed.
        Providing a specific time frame in which to perform the 
    surveillance test after attaining the required steam pressure ensures 
    that the test will be performed in a timely manner. The time frame 
    specified is consistent with NUREG-1431, Standard Technical 
    Specifications--Westinghouse Plants.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident.
        The proposed changes do not change system configurations, plant 
    equipment, or analysis. Therefore, the proposed changes will not 
    increase the possibility of a new or different kind of accident from 
    any accident previously identified.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to the minimum required steam pressure will not 
    affect the heat removal capability of the AFW System. Therefore, the 
    value assumed in the safety analysis is not changed. The change to the 
    specification 4.0.4 exemption to provide a specific time period does 
    not affect any margins of safety. Therefore, these changes do not 
    involve a significant reduction in any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: John F. Stolz.
    
    Public Service Electric & Gas Company
    
    Docket Nos. 50-272 and 50-311
    
        Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey.
        Date of amendment request: September 20, 1994.
        Description of amendment request: These proposed changes would 
    adopt the Westinghouse Standard Technical Specifications (NUREG-1431) 
    Channel Functional Test surveillance frequency for the Manual Reactor 
    Trip Switches and for the Reactor Trip Breakers (RTB) and relocate RTB 
    maintenance requirements from the Technical Specifications to the 
    Salem, Units 1 and 2, Updated Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed changes do not affect accident conditions or 
    assumptions. They change the existing surveillance test and their 
    frequencies to make them consistent with industry standards, and 
    relocate maintenance requirements to the UFSAR [Updated Final Safety 
    Analysis Report].
        The changes, for the Manual Reactor Trip Switch and Reactor Trip 
    Breaker (RTB) CHANNEL FUNCTIONAL TEST frequency, incorporate the 
    established Westinghouse STS surveillance frequencies. These 
    surveillance frequencies have received previous NRC review and generic 
    approval via the issuance of NUREG-1431. The Westinghouse STS does not 
    require Channel Functional Test for the Manual Reactor Trip Switches or 
    the RTB prior to each reactor startup.
        The addition of the RTB shunt trip feature for automatic reactor 
    trips, the improved RTB maintenance activities developed over the past 
    several years, and the implementation of 10 CFR 50.62 requirements have 
    improved RTB reliability. These features are unaffected by the proposed 
    changes. Excessive RTB testing results in increased component wear and 
    possibly reduced component life. Testing the RTBs with associated logic 
    trains reduces the potential for human errors and associated plant 
    transients.
        The consequences of accidents previously evaluated are unaffected 
    by the proposed changes.
        2. Does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed changes do not modify any system or equipment, nor 
    alter any process function. The Manual Reactor Trip Switch and RTB 
    functionality remains unchanged. Therefore these changes do not create 
    a new or un-evaluated accident or operating condition.
        3. Does not involve a significant reduction in a margin of safety.
        The proposed changes adopt the NRC approved Westinghouse STS 
    surveillance testing frequencies to maintain RTB reliability. Reduced 
    testing at power, consistent with the associated logic train test 
    frequency, reduces the potential for inadvertent actuation and 
    personnel errors. Thus, the proposed changes enhance plant safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502.
        NRC Project Director: John F. Stolz.
    
    Saxton Nuclear Experimental Corporation
    
    Docket No. 50-146
    
        Saxton Nuclear Facility, Bedford County, Pennsylvania.
        Date of amendment request: August 8, 1994. This supersedes the 
    request dated June 23, 1993.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications to allow characterization 
    activities related to the decommissioning of the Saxton Nuclear 
    Facility and add administrative activities associated with the 
    characterization activities.
        Basis for Proposed No Significant Hazards Consideration 
    Determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve a significant hazards 
    considerations because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The activities associated with characterization of the facility 
    will have a minimum impact on the physical condition of the containment 
    vessel as it relates to the risk of fire and has no effect on the risk 
    of flooding.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        In its present condition, the only accidents applicable to the site 
    are fire, flood, and radiological hazard. The possibility of a new or 
    different type of accident than that previously evaluated in the FSAR 
    will not be created by the implementation of activities permitted by 
    the approval of this amendment request.
        3. Involve a significant reduction in a margin of safety.
        No margins of safety relevant to the equipment at the facility 
    exist. Activities involved in characterization will not involve a 
    reduction in a margin of safety.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678.
        Attorney for the Licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts, and Trowbridge, 2300 N Street, NW, Washington, DC 
    20037.
        NRC Project Director: Seymour H. Weiss.
    
    Southern California Edison Company, et al.
    
    [Docket Nos. 50-361 and 50-362
    
        San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California.
        Date of amendment request: August 26, 1994.
        Description of amendment requests: The licensee proposes to revise 
    Technical Specification (TS) 3/4.7.5, ``Control Room Emergency Air 
    Cleanup System.'' The proposed revision to TS 3/4.7.5 will provide a 
    Limiting Condition of Operation (LCO) 3.0.4 exception for MODES 5, 6, 
    or a defueled configuration.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this proposed 
    change involve a significant increase in the probability or 
    consequences of any accident previously evaluated?
        Response: No.
        The Control Room Emergency Air Cleanup System (CREACUS) provides a 
    protected environment from which operators can control the plant 
    following an uncontrolled release of radioactivity or toxic gas.
        [The following are the proposed changes to Technical Specification 
    3/4.7.5 ``Control Room Emergency Air Cleanup System:'']
        Proposed Change 1 [adds the following statement to the 
    Applicability statement of TS 3.7.5: ``or during movement of irradiated 
    fuel assemblies.''] will replace the existing wording of the 
    Applicability with the following words ``ALL MODES or during movement 
    of irradiated fuel assemblies.'' The requirement concerning movement of 
    irradiated fuel assemblies was added because the existing Applicability 
    statement does not reflect the possibility of radiation exposure to the 
    operators inside the control room during this event. A fuel handling 
    accident can happen during defueled operations. In this case, movement 
    of the last irradiated fuel assembly from the empty core inside 
    containment is not covered by the existing Applicability.
        Also, a fuel handling accident can happen inside the Fuel Handling 
    Building when irradiated fuel is moved from one location to another in 
    the Spent Fuel Pool (SEP). The need for the CREACUS during fuel 
    handling is based on safety analysis assumptions which are specified in 
    Chapter 15 of the SONGS Unit 2 and 3 Updated Final Safety Analysis 
    Report (UFSAR).
        Addition of the new Applicability requirement will not involve a 
    significant increase in the possibility or consequences of any accident 
    previously evaluated.
        Proposed Change 2 [a new Action d): ``The provisions of 
    Specification 3.0.4 are not applicable when entering MODES 5, 6, or 
    defueled configuration'' is added to the Action section of TS 3.7.5] 
    will add a new Action d) which reads: ``the provisions of Specification 
    3.0.4 are not applicable when entering MODES 5, 6, or defueled 
    configuration.'' Existing Technical Specification 3/4.7.5 prohibits 
    entering MODE 6 from a defueled configuration unless both CREACUS 
    trains are OPERABLE. With the addition of the statement ``or during 
    movement of irradiated fuel assemblies'' to the Applicability, 
    OPERABILITY of the CREACUS will be ensured prior to movement of 
    irradiated fuel assemblies. Therefore, the only threshold between 
    defueled configuration and MODE 6 is the position of the first 
    irradiated fuel assembly--whether it is in the reactor vessel or 
    external to it. This threshold has no safety significance because the 
    only credible event during the transition from a defueled configuration 
    to MODE 6 and from MODE 6 to defueled configuration is a Design Basis 
    Fuel Handling Accident which is covered by the proposed Applicability. 
    Therefore, this threshold can be expected from Limiting Condition for 
    Operation (LCO) 3.0.4.
        The threshold of entering MODE 5 from MODE 6 consists of fully 
    tightening the last reactor vessel head closure bolt. This evolution 
    has no safety significance from the point of view of isolating the 
    control room from external hazards. Therefore, this MODE change can be 
    excepted from LCO 3.0.4. The threshold of entering MODE 6 from MODE 5 
    consists of untightening at least one reactor vessel head closure bolt. 
    If no irradiated fuel assemblies are being moved, this evolution has no 
    safety significance from the point of view of isolating the control 
    room from external hazards. Therefore, this MODE change can be excepted 
    from LCO 3.0.4 also.
        The threshold of entering MODE 5 from MODE 4 consists of decreasing 
    Reactor Coolant System (RCS) temperature from 350 deg.F > Tavg > 
    200 deg.F to Tavg [less than or equal to] 200 deg.F by initiating 
    shutdown cooling. If no irradiated fuel assemblies are being moved, 
    this evolution has no safety significance from the point of view of 
    isolating the control room from external hazards. Therefore, this MODE 
    change can be excepted from LCO 3.0.4.
        The MODE changes have no significance relative to releases. 
    Therefore, since CREACUS can be inoperable during each individual mode, 
    it should not be required to have two OPERABLE CREACUS trains before 
    mode changes.
        Therefore, addition of the new Action will not involve a 
    significant increase in the probability or consequences of any accident 
    previously evaluated.
        Proposed Change 3 [adds the following words ``or defueled 
    configuration when moving irradiated fuel assemblies'' after the words 
    ``Units 2 and 3 in MODE 5 or 6'' in the Action statement of TS 3.7.5] 
    will add the words ``or defueled when moving irradiated fuel 
    assemblies'' to the Action statement when either Unit is in MODE 5 or 
    6. These words are added for consistency with a proposed Applicability 
    statement ``or during movement of irradiated fuel assemblies.'' Without 
    these words it is not clear what Actions should be entered if the LCO 
    requirement is not met in a defueled configuration when moving 
    irradiated fuel assemblies. By adding these words Actions (a) and (b) 
    became applicable in a defueled configuration when moving irradiated 
    fuel assemblies. This change applies the requirement of the proposed 
    Applicability to the Action when either Unit is in MODES 5 or 6. 
    Therefore, addition of these words to the Action statement will not 
    involve a significant increase in the probability or consequences of 
    any accident previously evaluated.
        Proposed Change 4 [adds the following words ``or movement of 
    irradiated fuel assemblies'' after the words ``suspend all operations 
    involving CORE ALTERATIONS or positive reactivity changes'' in the 
    Action (b) statement of TS 3.7.5] will add the words ``or movement of 
    irradiated fuel assemblies'' in the Action (b) statement. These words 
    are added for consistency with the proposed Applicability statement and 
    proposed Action statement when either Unit is in MODES 5 or 6, or a 
    defueled configuration when moving irradiated fuel assemblies. Without 
    addition of these words Action (b) did not specify what should be done 
    when any Unit is in a defueled configuration when moving irradiated 
    fuel assemblies. Therefore, addition of these words to the Action 
    statement will not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. Will operation of the facility in accordance with this proposed 
    change create the possibility of a new or different kind of accident 
    from any previously evaluated?
        Response: No.
        The changes proposed herein do not reduce the reliability or 
    performance of the Control Room Emergency Air Cleanup System (CREACUS). 
    The proposed LCO 3.0.4 exception for CREACUS permits MODE 5, MODE 6, or 
    defueled configuration entry with one train of CREACUS inoperable. This 
    change does not affect CREACUS reliability and its capability to 
    perform its intended design functions.
        Additional requirements in the Applicability to have two Control 
    Room Emergency Air Cleanup Systems OPERABLE during movement of 
    irradiated fuel covers the consequences of a fuel accident in the Fuel 
    Handling Building and in containment when the reactor vessel is 
    defueled. Operation of the facility will remain unchanged as a result 
    of the proposed changes.
        Also, addition of the requirement to suspend movement of irradiated 
    fuel assemblies when either Unit is in a defueled configuration when 
    moving irradiated fuel is made for consistency with the proposed 
    Applicability statement and Action statement. The proposed Action 
    statement emphasize that Actions (a) and (b) are applicable not only 
    when either Unit is in MODES 5 or 6, but also when in a defueled 
    configuration when moving irradiated fuel assemblies. This change does 
    not affect CREACUS reliability and its capability to perform its 
    intended design functions. Therefore, the proposed changes will not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Will operation of the facility in accordance with this proposed 
    change involve a significant reduction in a margin of safety?
        Response: No.
        Operation of the facility in accordance with these changes will not 
    be adversely affected as a result of the changes proposed herein. The 
    proposed changes include a change to the Applicability, adding the new 
    Action (d), modifying the Action statement when either Unit is in MODES 
    5 or 6, and modifying the Action (b). The proposed LCO 3.0.4 exception 
    for CREACUS permits MODE 5, MODE 6, or defueled configuration entry 
    with one train of CREACUS inoperable. Additional requirements in the 
    Applicability statement to have two Control Room Emergency Air Cleanup 
    Systems OPERABLE during movement of irradiated fuel, covers the 
    consequences of the fuel accident in the Fuel Handling Building. Also, 
    this requirement covers the movement of irradiated fuel when the 
    reactor vessel is defueled. Modified Action statement for either Unit 
    in MODES 5 or 6 is made for consistency with the proposed Applicability 
    statement. Modified Action (b) covers the possibility of both the 
    CREACUS trains being inoperable in a defueled configuration when moving 
    irradiated fuel assemblies.
        The margin of safety as defined in Bases 3/4.7.5 is limiting the 
    dose to control room personnel to 5.0 rem or less whole body, or its 
    equivalent. As discussed above, operation of the CREACUS will be 
    unchanged as a result of the proposed changes. Therefore, operation of 
    the facility in accordance with this proposed change will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: Theodore R. Quay.
    
    Southern California Edison Company, et al.
    
    Docket Nos. 50-361 and 50-362.
    
        San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California.
        Date of amendment requests: September 16, 1994.
        Description of amendment requests: The licensee proposes to revise 
    the linear heat rate (LHR) limit in Technical Specification (TS) 3/
    4.2.1, ``Linear Heat Rate.'' TS 3/4.2.1 requires maintaining the LHR at 
    or below 13.9 kilowatts per linear foot (kw/ft) for steady-state 
    operation. This amendment request is to revise this value from 13.9 kw/
    ft to 13.0 kw/ft. The Bases of TS 3/4.2.1, ``Linear Heat Rate,'' are 
    also being revised to reflect the new value.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this proposed 
    change involve a significant increase in the probability or 
    consequences of any accident previously evaluated?
        Response: No.
        The only event impacted by this Technical Specification (TS) change 
    is the Large Break Loss of Coolant Accident (LBLOCA) which has been 
    reanalyzed. There is a direct correlation between the magnitude of the 
    TS 3/4.2.1 Linear Heat Rate (LHR) limit and the calculated peak 
    cladding temperature (PCT). Since the LHR is being reduced in value, 
    which is a conservative change, there will be no increase in the 
    consequences of the event. The LBLOCA reanalysis, performed using the 
    new LHR limit in support of an optimized fuel loading pattern, resulted 
    in a reduction of the calculated LBLOCA PCT. Therefore, this change 
    will not involve an increase in the probability or consequences of any 
    accident previously evaluated.
        2. Will operation of the facility in accordance with this proposed 
    change create the possibility of a new or different kind of accident 
    from any previously evaluated?
        Response: No.
        This amendment request does not involve any change to plant 
    equipment or operation. The linear heat rate limit provided in T/S 
    3.2.1 is used only in the LBLOCA analysis. No change to the LBLOCA 
    methodology was made. Therefore, this change does not create the 
    possibility of a new or different kind of accident from any previously 
    evaluated.
        3. Will operation of the facility in accordance with this proposed 
    change involve a significant reduction in a margin of safety?
        Response: No.
        This amendment does not change the manner in which safety limits, 
    limiting safety settings, or limiting conditions for operation are 
    determined. There is no change in the PCT acceptance criterion for this 
    event as a result of the proposed reduction in the LHR limit. 
    Therefore, there is no reduction in the margin of safety from the 
    acceptance limit to the mechanical failure point of the fuel. 
    Additionally, the analysis value for the LBLOCA PCT is reduced to 2160 
    deg.F. This results in an increase in the analysis margin between the 
    acceptance criterion and the analysis value. Therefore, this proposed 
    change does not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
        Attorney for licensee: T.E. Oubre, Esquire, Southern California 
    Edison Company, P.O. Box 800, Rosemead, California 91770.
        NRC Project Director: Theodore R. Quay.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company
    
    Docket No. 50-346
    
        Davis-Besse Nuclear Power Station, Unit No. 1, Ottawa County, Ohio.
        Date of amendment request: October 7, 1994.
        Description of amendment request: The proposed amendment would 
    remove the existing Surveillance Requirement (SR) 4.5.2.d.3 for the Low 
    Pressure Injection (LPI) System and the existing SR 4.6.2.1.c for the 
    Containment Spray (CS) System since the requirement to leak test these 
    systems is programmatically covered in TS 6.8.4.a, ``Primary Coolant 
    Sources Outside Containment.'' Additionally, changes are proposed to TS 
    Bases 3/4.5.2 and 3/4.6.2.1 to reflect the elimination of the above 
    SRs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the NRC staff has 
    reviewed the licensee's analysis against the standards of 10 CFR 
    50.92(c). The staff's review is presented below:
        (1) The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The change does not involve a significant increase in the 
    probability of an accident previously evaluated nor does it involve a 
    significant increase in the consequences of an accident previously 
    evaluated because no accident initiators, conditions or assumptions are 
    affected by removing the leak test requirements of LPI System SR 
    4.5.2.d.3 and CS System SR 4.6.2.1.c. The purpose of these SRs is 
    already encompassed by the existing program requirements of TS 6.8.4.a, 
    ``Primary Coolant Sources Outside Containment.'' TS 6.8.4.a requires 
    integrated leak testing at refueling cycle intervals or less, for each 
    system outside containment, that could contain highly radioactive 
    fluids during a serious transient or accident.
        The proposed changes do not alter the source term, containment 
    isolation, or allowable releases. The proposed changes, therefore, will 
    not increase the radiological consequences of a previously evaluated 
    event.
        These changes are consistent with NUREG-1430, Revision 0, 
    ``Improved Standard Technical Specifications for B&W Plants.'' The 
    associated changes to TS Bases 3/4.5.2 and 3/4.6.2.1 are 
    administrative.
        (2) The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not create the possibility of any new or 
    different kind of accident from any accident previously evaluated 
    because no new accident initiators or assumptions are introduced by 
    these proposed changes to LPI System SR 4.5.2.d.3 and CS System SR 
    4.6.2.1.c. The purpose of these SRs is already encompassed by the 
    existing program requirements of TS 6.8.4.a, ``Primary Coolant Sources 
    Outside Containment,'' which requires leak testing to be performed on 
    the LPI and CS Systems. These changes are consistent with NUREG-1430. 
    The associated changes to TS Bases 3/4.5.2 and 3/4.6.2.1 are 
    administrative. The proposed changes do not alter any accident 
    scenarios.
        (3) The proposed changes do not result in a significant reduction 
    in the margin of safety.
        The changes do not involve a significant reduction in the margin of 
    safety because the proposed changes to the LPI System SR 4.5.2.d.3 and 
    CS System SR 4.6.2.1.c do not reduce or adversely affect the 
    capabilities of any plant structures, systems or components. The 
    purpose of these SRs is already encompassed by the existing program 
    requirements of TS 6.8.4.a, ``Primary Coolant Sources Outside 
    Containment.'' These changes are consistent with NUREG-1430. The 
    associated changes to TS Bases 3/4.5.2 and 3/4.6.2.1 are 
    administrative.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Acting Project Director: C.A. Carpenter.
    
    Virginia Electric and Power Company
    
    Docket Nos. 50-280 and 50-281
    
        Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
        Date of amendment request: October 11, 1994.
        Description of amendment request: The proposed changes would modify 
    the surveillance frequencies of the containment hydrogen analyzers.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of Surry Power Station in accordance with 
    the proposed Technical Specifications will not:
        1. Involve a significant increase in the probability of occurrence 
    or consequences of an accident previously evaluated.
        The proposed changes to the surveillance requirements for the 
    hydrogen analyzers have no impact on the probability of any accident 
    occurrence. The hydrogen analyzers are maintained in a standby mode 
    during normal operation and are made fully operable within thirty 
    minutes after a safety injection signal to provide indication of the 
    hydrogen concentration in containment after a loss-of-coolant accident. 
    This instrumentation is used solely post-accident to monitor 
    containment conditions. Reduced testing of a post-accident monitor does 
    not contribute to the probability of any previously analyzed accident. 
    These monitors have no automatic safety function. Furthermore, the 
    hydrogen analyzers will be operated in the same manner, and the 
    operability requirements are not being altered. In addition, the Post-
    Accident Sampling System serves as a diverse means to confirm post-
    accident hydrogen concentration in containment. Therefore, the 
    consequences of a Design Basis Accident are not being increased by the 
    proposed change in surveillance test frequency of the hydrogen 
    analyzers.
        Reducing the frequency of surveillance testing could however 
    decrease the timeliness in identifying an inoperable hydrogen analyzer. 
    However, our surveillance test experience has shown that the analyzers 
    have been very stable with repeatable results, and we conclude that the 
    change in test frequency should not affect the reliability or 
    operability of the analyzers. Likewise, the NRC has determined in 
    Generic Letter 93-05 that a reduced frequency of surveillance testing 
    during power is acceptable to determine hydrogen analyzer operability.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        There are no plant modifications or changes in methods of plant 
    operation introduced by this change in hydrogen analyzer surveillance 
    frequencies. The hydrogen analyzers are maintained in a standby mode 
    during normal operation and are fully operable within thirty minutes 
    after a safety injection signal to provide indication of the hydrogen 
    concentration in containment after a loss-of-coolant accident. 
    Therefore, the possibility of a new or different kind of accident than 
    previously evaluated is not created by the proposed changes in 
    surveillance frequency of the control rods [hydrogen analyzers 
    surveillance frequencies].
        3. Involve a significant reduction in a margin of safety.
        The hydrogen analyzer surveillance requirements do not affect the 
    margin of safety in that the operability requirements for the safety 
    systems and containment remain unchanged. The hydrogen analyzers only 
    provide indication and do not perform any direct function to mitigate 
    the consequences of any previously analyzed accidents. Furthermore, the 
    change in surveillance frequency is associated with a post-accident 
    monitor with no automatic safety functions and a diverse means of 
    confirming the parameter by the Post-Accident Sampling System. 
    Therefore, the margin of safety is not altered by this proposed change 
    in the surveillance frequencies of the hydrogen analyzers.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Mohan C. Thadani (Acting).
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Northeast Nuclear Energy Company, et al.
    
    Docket No. 50-336
    
        Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut.
        Date of amendment request: September 26, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications by adding a footnote to 
    Surveillance Requirement 4.6.1.2.d that defers the performance of Type 
    B and C containment leak rate tests to the end of the twelfth refueling 
    outage.
        Date of publication of individual notice in Federal Register: 
    October 13, 1994, (59 FR 52005).
        Expiration date of individual notice: November 14, 1994.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community--Technical College, Thames Valley Campus, 574 
    New London Turnpike, Norwich, CT 06360.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Arizona Public Service Company, et al.
    
    Docket Nos. STN 50-528, STN 50-529, and STN 50-530
    
        Palo Verde Nuclear Generating Station, Units 1, 2, and 3, Maricopa 
    County, Arizona.
        Date of application for amendments: August 23, 1993, as 
    supplemented by letter of July 21, 1994.
        Brief description of amendments: These amendments remove the Units 
    1 and 3 license condition regarding an augmented reactor coolant pump 
    vibration monitoring program and the confirmatory order modifying the 
    Unit 2 license regarding the same issue.
        Date of issuance: October 27, 1994.
        Effective date: October 27, 1994.
        Amendment Nos.: 84, 72, and 56.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 29, 1993 (58 
    FR 50963).
        The additional information in the letter dated July 21, 1994, was 
    clarifying in nature and did not affect the staff's previously 
    published no significant hazards determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 27, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Baltimore Gas and Electric Company
    
    Docket Nos. 50-317 and 50-318
    
        Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 & 2, Calvert 
    County, Maryland.
        Date of application for amendments: August 4, 1994.
        Brief description of amendments: The amendments delete Technical 
    Specifications 3/4.3.3.3, 6.9.2.b, 6.9.2.d, and Bases 3/4.3.3.3, which 
    provide the requirements for the operation and the testing of seismic 
    monitoring instrumentation, and relocates them to the Updated Final 
    Safety Analysis Report and plant procedures.
        Date of issuance: October 21, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 199 and 176
        Facility Operating License No. DPR-53 and DPR-69: Amendment revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47165).
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated October 21, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company
    
    Docket Nos. 50-317 and 50-318
    
        Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland.
        Date of application for amendments: November 4, 1993.
        Brief description of amendments: These amendments revise the 
    Updated Final Safety Analysis Report to address the removal of orifice 
    plates in the containment vent/purge lines of each unit and revise the 
    maximum hypothetical accident analysis to address the increased flow as 
    the result of removing the orifice plates.
        Date of issuance: October 21, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 200 and 177.
        Facility Operating License No. DPR-53 and DPR-69: Amendment revised 
    the Licenses.
        Date of initial notice in Federal Register: February 25, 1994 (59 
    FR 9254).
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated October 21, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Commonwealth Edison Company
    
    Docket Nos. STN 50-454 and STN 50-455
    
        Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois.
        Date of application for amendments: August 1, 1994, as supplemented 
    by your letters dated September 7, 1994, and September 17, 1994 (two 
    letters), with clarifying information submitted by letters dated 
    September 22, 1994, September 23, 1994, September 30, 1994, October 17, 
    1994, and October 24, 1994.
        Brief description of amendments: The purpose of the amendment is to 
    incorporate voltage-based repair criteria into the Byron, Unit 1, 
    technical specifications, thereby permitting the use of voltage-based 
    steam generator (SG) tube plugging criteria for a specific class of SG 
    tube defects.
        Date of issuance: October 24, 1994.
        Effective date: October 24, 1994.
        Amendment Nos.: 66 and 66.
        Facility Operating License Nos. NPF-37 and NPF-66: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 23, 1994 (59 
    FR 48917).
        The clarifying information in the September 22, 1994, September 23, 
    1994, September 30, 1994, October 17, 1994, and October 24, 1994, 
    submittals did not affect the initial determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated October 24, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Byron Public Library, 109 N. 
    Franklin, P.O. Box 434, Byron, Illinois 61010.
    
    Commonwealth Edison Company
    
    Docket Nos. STN 50-454 and STN 50-455
    
        Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois.
    
    Docket Nos. STN 50-456 and STN 50-457
    
        Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois.
        Date of application for amendments: March 23, 1994, as supplemented 
    on July 26, 1994.
        Brief description of amendments: The amendments change the 
    Technical Specifications to reflect a reduced thermal flow to 
    compensate for increased steam generator tube plugging up to 15 percent 
    of the total number of tubes. The amendment also approves the use of 
    higher boron concentration in the refueling water storage tank, the 
    reactor coolant system accumulators, and the refueling cavity.
        Date of issuance: October 21, 1994.
        Effective date: October 21, 1994.
        Amendment Nos.: 65, 65, 56, and 55.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: August 15, 1994 (59 FR 
    41802).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 21, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Consumers Power Company
    
    Docket No. 50-255
    
        Palisades Plant, Van Buren County, Michigan.
        Date of application for amendment: November 15, 1991, supplemented 
    February 22, March 11, April 7, and August 23, 1994.
        Brief description of amendment: This amendment is a complete 
    rewrite of the instrumentation operability requirements.
        Date of issuance: October 26, 1994.
        Effective date: October 26, 1994.
        Amendment No.: 162.
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27052)
        The August 23, 1994, request contained editorial changes within the 
    scope of the initial notice and did not affect the staff's proposed no 
    significant hazards consideration findings. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    October 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
    
    Entergy Operations, Inc.,
    
    Docket No. 50-313
    
        Arkansas Nuclear One, Unit No. 1, Pope County, Arkansas.
        Date of amendment request: January 13, 1994.
        Brief description of amendment: The amendment revised the 
    specifications governing the reactor protection system (RPS) to permit 
    the plant to operate indefinitely with one RPS channel in by-pass.
        Date of issuance: October 24, 1994.
        Effective date: October 24, 1994.
        Amendment No.: 174.
        Facility Operating License No. DPR-51. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10005).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 24, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    Florida Power and Light Company
    
    Docket Nos. 50-250 and 50-251
    
        Turkey Point Plant Units 3 and 4, Dade County, Florida.
        Date of application for amendments: February 18, 1994, as 
    supplemented by letter dated August 5, 1994.
        Brief description of amendments: These amendments delete the audit 
    frequencies from the Technical Specifications (TS) and modify the TS 
    administrative control requirements for emergency and security plans.
        Date of issuance: October 26, 1994.
        Effective date: October 26, 1994.
        Amendment Nos: 168 and 162.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14889). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated October 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    GPU Nuclear Corporation, et al.
    
    Docket No. 50-219
    
        Oyster Creek Nuclear Generating Station, Ocean County, New Jersey.
        Date of application for amendment: August 19, 1994.
        Brief description of amendment: The amendment updates and clarifies 
    the surveillance requirements for control rod exercising and standby 
    liquid control pump operability testing to be consistent with Generic 
    Letter 93-05.
        Date of Issuance: October 19, 1994.
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 172.
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47168).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated October 19, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    IES Utilities Inc.
    
    Docket No. 50-331
    
        Duane Arnold Energy Center, Linn County, Iowa.
        Date of application for amendment: May 28, 1992, as supplemented on 
    January 6, May 27 and October 20, 1994.
        Brief description of amendment: The amendment revised the Technical 
    Specifications by changing the limiting conditions for operation and 
    surveillance requirements for primary containment integrity, secondary 
    containment integrity, and other systems and equipment of Section 3.7, 
    Containment Systems. Limiting conditions for operation and surveillance 
    requirements for drywell average air temperature and secondary 
    containment automatic isolation dampers were also added.
        Date of issuance: October 26, 1994.
        Effective date: October 26, 1994, to implemented within 120 days.
        Amendment No.: 201
        Facility Operating License No. DPR-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 6, 1994 (59 FR 
    34665). The licensee's October 20, 1994, submittal, provided clarifying 
    information at the request of the NRC staff. This submittal did not 
    change the initial application or the no significant hazards 
    determination as originally noticed. Therefore, renoticing was not 
    warranted.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401.
    
    Northeast Nuclear Energy Company, et al.
    
    Docket No. 50-423
    
        Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut.
        Date of application for amendment: September 30, 1993, as 
    supplemented July 8, 1994.
        Brief description of amendment: The amendment revises the Technical 
    Specifications by increasing the minimum volume of fuel oil required to 
    be stored in the emergency diesel generator (EDG) day tank from 205 
    gallons to 278 gallons, and clarifies the bases for the EDG fuel oil 
    storage tank and day tank minimum fuel oil volume requirements.
        Date of issuance: October 17, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 97.
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59753).
        The July 8, 1994, letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 17, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Pennsylvania Power and Light Company
    
    Docket Nos. 50-387 and 50-388
    
        Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania.
        Date of application for amendments: May 31, 1994.
        Brief description of amendments: These amendments change the 
    frequency for monitoring the Susquehanna site spray pond ground water 
    level from once per month to once every 6 months.
        Date of issuance: October 20, 1994.
        Effective date: Both units; as of date of issuance and to be 
    implemented within 30 days after the date of issuance.
        Amendment Nos.: 135 and 105.
        Facility Operating License Nos. NPF-14 and NPF-22. These amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 6, 1994 (59 FR 
    34668).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 20, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Public Service Electric and Gas Company 
    Delmarva Power and Light Company, and Atlantic City Electric Company
    
    Docket No. 50-277
    
        Peach Bottom Atomic Power Station, Unit No. 2, York County, 
    Pennsylvania.
        Date of application for amendment: June 23, 1993, as supplemented 
    by letters dated April 5, May 2, June 6, June 8, July 6 (two letters), 
    July 7, July 20, July 28, 1994 (two letters), September 16, September 
    30, and October 14, 1994. The supplemental letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        Brief description of amendment: The amendment raises the authorized 
    maximum power level from 3293 MWt to a new limit of 3458 MWt.
        Date of issuance: October 18, 1994.
        Effective date: Unit 2, effective as of its date of issuance and is 
    to be implemented prior to startup in Cycle 11 currently scheduled for 
    October 28, 1994.
        Amendment No.: 198.
        Facility Operating License No. DPR-44: The amendment revised the 
    license and Technical Specifications.
        Date of initial notice in Federal Register: August 29, 1994 (59 FR 
    44432).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 18, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Public Service Electric & Gas Company
    
    Docket Nos. 50-272 and 50-311
    
        Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey.
        Date of application for amendments: February 18, as supplemented by 
    letter dated April 6, 1994 for Salem Unit 1 and March 28, 1994 for 
    Salem Unit 2.
        Brief description of amendments: The change to Salem Unit 1 
    Technical Specifications (TS) replaces the main feedwater control and 
    control bypass valves with the main feedwater stop check valves for the 
    Containment Isolation Function. The change to Salem Unit 2 TS adds a 
    footnote to the 21-24 BF22 (main feedwater stop check valves) on Table 
    3.6-1, ``Containment Isolation Valves.'' This note identifies those 
    containment isolation Valves that are not subject to 10 CFR Part 50, 
    Appendix J, Type C leakage testing.
        Date of issuance: October 20, 1994.
        Effective date: Units 1 and 2, effective as of date of issuance and 
    shall be implemented within 60 days of the date of issuance.
        Amendment Nos.: 158 and 139.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37083).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 20, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    Southern California Edison Company, et al.
    
    Docket Nos. 50-361 and 50-362
    
        San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California
        Date of application for amendments: December 31, 1992.
        Brief description of amendments: These amendments revise the 
    Technical Specifications (TS) to (1) distinguish between the core 
    operating limit supervisory system (COLSS) in service and the COLSS out 
    of service (OOS), (2) add surveillances to monitor departure from 
    nucleate boiling ratio (DNBR) and/or linear heat rate (LHR) every 15 
    minutes when the COLSS is OOS and the corresponding parameter is not 
    being maintained as required, (3) increase the ACTION time from 1 hour 
    to 4 hours when the COLSS is OOS and either the LHR or DNBR margin is 
    not being maintained within the required limits, (4) change the power 
    reduction requirements from ``HOT STANDBY'' to ``less than or equal to 
    20 percent of Rated Thermal Power'' when the DNBR margin and/or the LHR 
    limiting condition for operation (LCO) cannot be met within the allowed 
    ACTION time, and (5) revise the Bases to the TS to reflect these 
    changes.
        Date of issuance: October 27, 1994.
        Effective date: October 27, 1994.
        Amendment Nos.: 113 and 102.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 3, 1993 (58 FR 
    12269).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated October 27, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
    
    Tennessee Valley Authority
    
    Docket Nos. 50-327 and 50-328
    
        Sequoyah Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee.
        Date of application for amendments: May 18, 1994; revised September 
    9, 1994 (TS 94-05).
        Brief description of amendments: The amendments revise the action 
    statement to provide a fixed duration that the control room emergency 
    ventilation system may be inoperable due to actions taken as a result 
    of a tornado warning.
        Date of issuance: October 17, 1994.
        Effective date: October 17, 1994.
        Amendment Nos.: 187 and 179.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: June 22, 1994 (59 FR 
    32237).
        The Commission's related evaluation of the amendments are contained 
    in a Safety Evaluation dated October 17, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Tennessee Valley Authority
    
    Docket Nos. 50-327 and 50-328
    
        Sequoyah Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee.
        Date of application for amendments: August 19, 1994 (TS 93-09).
        Brief description of amendments: The amendments delay 
    implementation of Amendments Nos. 182 and 174 from the Unit 2 Cycle 6 
    refueling outage to as soon as acceptable plant conditions and 
    modification activities/procedures are established in fiscal year 1995.
        Date of issuance: October 17, 1994.
        Effective date: October 17, 1994.
        Amendment Nos.: 188 and 180.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47182).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 17, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Tennessee Valley Authority
    
    Docket Nos. 50-327 and 50-328
    
        Sequoyah Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee.
        Date of application for amendments: September 8, 1994 (TS 94-14).
        Brief description of amendments: The amendments incorporate 
    clarifications regarding the evaluation of steam generator tube defects 
    by separating the portion of the steam generator tube starting at the 
    end of the tube up to the start of the tube-to-tube sheet weld from the 
    remainder of the tube for the purposes of sample selection and repair 
    when defects are found in this section of a steam generator tube.
        Date of issuance: October 20, 1994.
        Effective date: October 20, 1994.
        Amendment Nos.: 189 and 181.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: September 19, 1994. (59 
    FR 47962).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 20, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company
    
    Docket No. 50-346
    
        Davis-Besse Nuclear Power Station, Unit No. 1, Ottawa County, Ohio.
        Date of application for amendment: April 5, 1994.
        Brief description of amendment: The amendment increases the 
    surveillance test interval for the turbine-driven auxiliary feedwater 
    pump and motor-driven feedwater pump from 31 days to 92 days; clarifies 
    a requirement for a dedicated individual to be stationed at manual 
    valves during surveillance testing because of the availability of the 
    motor-driven feedwater system; addresses miscellaneous editorial 
    corrections, and revises TS 3/4.7.1.2 and TS 3/4.1.7 and their 
    associated bases.
        Date of issuance: October 18, 1994.
        Effective date: October 18, 1994.
        Amendment No.: 193.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27068).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 18, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Union Electric Company
    
    Docket No. 50-483
    
        Callaway Plant, Unit 1, Callaway County, Missouri.
        Date of application for amendment: February 10, 1994.
        Brief description of amendment: The amendment revises the Technical 
    Specification Table 2.2-1, ``Reactor Trip System Instrumentation Trip 
    Setpoints,'' to correct Total Allowance values. The associated Bases 
    section clarifies the relationship between the power supply and 
    undervoltage relays.
        Date of issuance: October 27, 1994.
        Effective date: Date of issuance to be implemented within 30 days.
        Amendment No.: 93.
        Facility Operating License No. NPF-30. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14897).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 27, 1994.
        No Significant hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Vermont Yankee Nuclear Power Corporation
    
    Docket No. 50-271
    
        Vermont Yankee Nuclear Power Station, Vernon, Vermont.
        Date of application for amendment: December 6, 1993.
        Brief description of amendment: The proposed change removes the 
    requirement to perform jet pump integrity and operability surveillances 
    in the idle loop during operation with one recirculation loop.
        Date of issuance: October 26, 1994.
        Effective date: October 26, 1994.
        Amendment No.: 141.
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29637).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, Vermont 05301.
    
    Virginia Electric and Power Company
    
    Docket Nos. 50-280 and 50-281
    
        Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
        Date of application for amendments: October 19, 1993.
        Brief description of amendments: These amendments will add 
    operability requirements, action statements, and surveillance 
    requirements for the recirculation spray heat exchanger service water 
    outlet radiation monitors. Also, surveillance requirements for several 
    post-accident instruments are being reinstated.
        Date of issuance: October 27, 1994.
        Effective date: October 27, 1994.
        Amendment Nos.: 193 and 193.
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67864).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated October 27, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By December 9, 1994, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
    
    Wisconsin Electric Power Company
    
    Docket Nos. 50-266 and 50-301
    
        Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin.
        Date of application for amendments: October 20, 1994.
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) Section 15.3.1.G, ``Operational Limitations,'' to 
    reduce the reactor coolant system raw measured total flow rate and 
    operating pressure, modify TS Section 15.2.3.1.B to increase the 
    required reduction in the delta-T trip setpoint, and modify TS Figure 
    15.2.1-1 to reflect new reactor core safety limits, all for Unit 2 
    only. The applicable bases are also revised.
        Date of issuance: October 28, 1994.
        Effective date: October 28, 1994.
        Amendment Nos.: 156 and 160.
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated 
    October 28, 1994.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Ernest L. Blake, Jr., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037.
        Acting NRC Project Director: Cynthia A. Carpenter.
    
        Dated at Rockville, Maryland, this 2nd day of November, 1994.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 94-27613 Filed 11-8-94; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
11/09/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-27613
Dates:
October 27, 1994.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: November 9, 1994