96-31944. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 244 (Wednesday, December 18, 1996)]
    [Notices]
    [Pages 66702-66721]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-31944]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from November 22, 1996, through December 6, 1996. 
    The last biweekly notice was published on December 4, 1996.
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By January 17, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one
    
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    contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois Docket 
    Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 1 and 
    2, Rock Island County, Illinois
    
        Date of application for amendment request: September 20, 1996.
        Description of amendment request: The proposed amendments would 
    update the Pressure Temperature (P-T) curves contained in the Technical 
    Specifications to 22 Effective Full Power Years (EFPYs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because of the 
    following:
        The proposed changes merely adjust the reference temperature for 
    the limiting beltline material to account for irradiation effects 
    and provide the same level of protection as previously evaluated. 
    The adjusted reference temperature calculations were performed 
    utilizing the guidance contained in Regulatory Guide 1.99, Revision 
    2. The change is administrative in nature to reflect the extension 
    of the operating limits to 22 EFPY. As such, these changes will not 
    significantly increase the probability or consequences of a 
    previously evaluated accident.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        The proposed changes do not create the possibility of a new or 
    different kind of accident previously evaluated for Dresden or Quad 
    Cities Stations. No new modes of operation are introduced by the 
    proposed changes. The revised operating limits are merely an update 
    of the old limits by taking into account the effects of irradiation 
    on the limiting reactor vessel material. Use of the revised P-T 
    curves will continue to provide the same level of protection as was 
    previously reviewed and approved. Therefore, the proposed changes do 
    not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The associated change to the P-T curves related to this proposed 
    amendment does not affect any activities or equipment and are not 
    assumed in any safety analysis to initiate any accident sequence for 
    Dresden or Quad Cities Stations; therefore, the proposed changes do 
    not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        3. Involve a significant reduction in the margin of safety 
    because:
        The proposed amendment reflects an update of the P-T curves to 
    extend the operating limit to 22 EFPY. The revised curves are based 
    on the latest NRC guidance along with actual data for the units. The 
    new limits retain the margin of safety to the level expected for a 
    new vessel, adjusted for irradiation effects as required by 10 CFR, 
    Appendix G, thereby maintaining a conservative margin of safety.
        Therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: October 31, 1996.
        Description of amendment request: The proposed amendments would 
    relocate the requirements for seismic monitoring instrumentation from 
    the Technical Specifications to licensee controlled documents. The 
    Technical Specifications affected are 3/4.3.7.2, ``Seismic Monitoring 
    Instrumentation,'' Table 3.3.7.2-1, ``Seismic Monitoring 
    Instrumentation,'' Table 4.3.7.2-1, ``Seismic Monitoring 
    Instrumentation Surveillance Requirements,'' and Bases Section 3/
    4.3.7.2, ``Seismic Monitoring Instrumentation.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    
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        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        The function of the seismic monitoring instrumentation is to 
    monitor seismic activity above the Operating-Basis Earthquake (OBE) 
    threshold, and to record observed seismic data for comparison to 
    design basis response spectra. The seismic monitoring 
    instrumentation does not provide any function to mitigate an 
    accident or the consequences of an accident. The replacement seismic 
    monitoring instrumentation will remain in place. The proposed 
    Amendment is not a result of any changes to system function, alarm 
    setpoints, or main control room annunciators. Rather, the Technical 
    Specification requirements (as revised for the replacement 
    instrumentation) are being relocated to licensee-controlled 
    documents in accordance with NRC Generic Letter 95-10.
        The proposed change relocates requirements and surveillances for 
    structures, systems, components or variables that do not meet the 
    criteria for inclusion in Technical Specifications as identified in 
    the Application of Selection Criteria to the LaSalle Technical 
    Specifications. The affected structures, systems, components or 
    variables are not assumed to be initiators of analyzed events and 
    are not assumed to mitigate accident or transient events. The 
    requirements and surveillances for these affected structures, 
    systems, components or variables will be relocated from the 
    Technical Specifications to an appropriate administratively 
    controlled document which will be maintained pursuant to 10 CFR 
    50.59. In addition, the affected structures, systems, components or 
    variables are addressed in existing surveillance procedures which 
    are also controlled by 10 CFR 50.59 and subject to the change 
    control provisions imposed by plant administrative procedures, which 
    endorse applicable regulations and standards. Therefore, this change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        The seismic monitoring instrumentation does not provide any 
    function to mitigate an accident or the consequences of an accident. 
    The replacement seismic monitoring instrumentation will remain in 
    place and will provide the same basic function as the existing 
    instrumentation. The replacement instrumentation will provide 
    enhanced system reliability and will not result in any changes to 
    system function, alarm setpoints, or main control room annunciators. 
    The Technical Specification requirements (as revised for the 
    replacement instrumentation) are being relocated to licensee-
    controlled documents in accordance with NRC Generic Letter 95-10.
        The proposed change does not involve any change in the methods 
    governing normal plant operation. The proposed change will not 
    impose or eliminate any requirements and adequate control of 
    existing requirements will be maintained. Thus, this change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        (3) Involve a significant reduction in the margin of safety 
    because:
        The replacement seismic monitoring instrumentation will have no 
    impact on margin of safety. The intended function of the seismic 
    monitoring instrumentation, i.e. to record observed seismic data for 
    analysis to determine the impact on plant components, will be made 
    more reliable by this modification. The Technical Specification 
    requirements (as revised for the replacement instrumentation) are 
    being relocated to licensee-controlled documents in accordance with 
    NRC Generic Letter 95-10.
        The proposed change will not reduce a margin of safety because 
    it has no impact on any safety analysis assumptions. In addition, 
    the relocated requirements and surveillances for the affected 
    structure, system, component or variable continue to meet the same 
    requirements as the existing Technical Specifications. However, the 
    LCO requirement specified in Section 3.3.7.2.a (to prepare and 
    submit a Special Report to the NRC within 10 days of the seismic 
    monitoring instrumentation being inoperable for more than 30 days) 
    will not be included in the ATR [Administrative Technical 
    Requirements] since the Technical Specification Special Report 
    requirements are only applicable to the LCOs. Since any future 
    changes to these requirements or the surveillance procedures will be 
    evaluated per the requirements of 10 CFR 50.59, no reduction in a 
    margin of safety will be permitted.
        The existing requirement for NRC review and approval of 
    revisions, in accordance with 10 CFR 50.92, to these details 
    proposed for relocation does not have a specific margin of safety 
    upon which to evaluate. However, since the proposed change is 
    consistent with the BWR Standard Technical Specification, NUREG-
    1434, Rev. 1 approved by the NRC Staff, revising the Technical 
    Specifications to reflect the approved level of detail ensures no 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: November 7, 1996.
        Description of amendment request: The proposed amendments would 
    change Specification 4.3.1.A.4.b from verifying greater than or equal 
    to 17 percent steam generator secondary side wide range water level to 
    greater than or equal to 17 percent steam generator secondary side 
    narrow range water level.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of occurrence of any accident 
    previously evaluated.
        Maintaining secondary side steam generator water level greater 
    than or equal to 17 percent by wide range level indication is the 
    current requirement by the technical specifications. By revising the 
    requirement to require using the narrow range water level, no change 
    in operating practices or plant configuration is made. The minimum 
    requirement of 17 percent by narrow range level indication is more 
    restrictive and conservative than 17 percent by wide range 
    indication. The requirement to maintain secondary side steam 
    generator water level greater than or equal to 17 percent by narrow 
    range indication is currently required by operations procedure PT-O, 
    Appendix F-1 and will be maintained. This change ensures that the 
    requirements for natural circulation cooldown are maintained in Mode 
    4. Therefore, changing this surveillance requirement does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not require a physical alteration of the 
    plant (no new or different equipment will be installed). The 
    Technical Specifications will continue to require OPERABLE steam 
    generator(s) for heat removal functions. The Technical 
    Specifications will continue to require the performance of SR 
    4.3.1.A.4.b. Changing the SR to use narrow level indication 
    correctly states the steam generator water level required to support 
    heat removal function. Thus, this change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not result in a significant reduction in 
    a margin of safety because it has no impact on any safety analysis 
    assumptions. The requirement to have OPERABLE steam generator(s) in 
    MODE 4 for heat removal function is maintained. The requirement to 
    perform SR 4.3.1.A.4.b is not changed. Changing the SR to use narrow 
    level indication correctly states the steam generator water level 
    required to support heat
    
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    removal function. Therefore, this change does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: November 7, 1996.
        Description of amendment request: The proposed amendments would 
    change the values for the reduced power range neutron flux high 
    setpoint trip that are specified when one or more code main steam 
    safety valves are inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of occurrence of any accident 
    previously evaluated.
        The requirement to change the Power Range Neutron Flux High Trip 
    setpoints to the Reduced Setpoint Values of Table 3.7-1 for the most 
    restrictive loop if one or more code MSSVs are inoperable is not 
    changed by this amendment. As such, no change in operating practices 
    or plant configuration is being made.
        The amendment provides new reduced setpoint values for the Power 
    Range Neutron flux High Trip to ensure that for the limiting 
    transient (Loss of Load/Turbine Trip [LOL/TT]), a secondary side 
    overpressurization condition does not occur. The new values were the 
    result of calculation using an algorithm provided by Westinghouse in 
    Westinghouse Nuclear Safety Advisory Letter NSAL-94-001, ``Operation 
    at Reduced Power Levels with Inoperable MSSVs,'' January 25, 1994. 
    The new values are much more restrictive than the previous values 
    and ensure that the probability or consequences of an accident 
    previously evaluated is not increased. Therefore, the new reduced 
    setpoint values do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not require a physical alteration of 
    the plant (no new or different equipment will be installed to 
    implement this change). The Reduced Neutron Flux High Trip setpoints 
    ensure that a secondary side overpressurization transient does not 
    occur for the most limiting transient. In addition, no new modes of 
    operations will be introduced by this change. Thus, this change does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        This amendment provides new Reduced Power Range Neutron Flux 
    High Trip setpoints.The Specification that requires the Power Range 
    Neutron Flux High Trip setpoints be changed to the reduced values 
    for one or more inoperable MSSVs is not changed. The reduced Trip 
    setpoints are the result of new calculations using an algorithm 
    provided by Westinghouse in Westinghouse Nuclear Safety Advisory 
    Letter NSAL-94-001, ``Operation at Reduced Power levels with 
    Inoperable MSSVs,'' January 25, 1994, and ensure the LOL/TT 
    transient does not result in a secondary overpressurization. 
    Therefore, this change does not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: November 7, 1996.
        Description of amendment request: The proposed amendments would 
    clarify the operability requirements for the residual heat removal 
    (RHR) loops during core alteration operations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of occurrence of any accident 
    previously evaluated.
        The ability to remove an RHR loop from operation for up to one 
    hour per eight-hour period is currently allowed by technical 
    specification 3.13.9.B.b. By adding a reference to LCO [Limiting 
    Condition for Operation] 3.13.1.A.4. and adding the requirement to 
    suspend CORE ALTERATIONS to Action 3.13.9.B.a. to be consistent with 
    3.13.9.B.b., no change in operating practices or plant configuration 
    is made. By maintaining the requirement to have an RHR loop in 
    operation during MODE 6, and by requiring CORE ALTERATIONS to be 
    suspended if an RHR loop is not back in operation after one hour, 
    adequate corrective actions are implemented until the RHR loop is 
    restored to operating status. Therefore, operation of the system is 
    consistent with current technical specifications and this change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not require a physical alteration of the 
    plant (no new or different equipment will be installed to implement 
    this change). The Technical Specifications will continue to require 
    an RHR loop to be in operation during MODE 6, and will only permit 
    the loop to be not in operation for up to one hour in an eight-hour 
    period. The Technical Specifications will continue to require 
    compliance with these limitations and suspension of CORE ALTERATIONS 
    if an RHR loop is not in operation for more than one hour. Thus, 
    this change does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not result in a significant reduction in 
    a margin of safety because it has no impact on any safety analysis 
    assumptions. The requirement to have an RHR loop in operation during 
    MODE 6 is maintained, along with the ability to remove RHR from 
    operation for up to one hour per eight-hour period. If an RHR loop 
    is not in service beyond 1 hour per TS 3.13.9.B, CORE ALTERATIONS 
    will be suspended. Therefore, this change does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One
    
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    First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of amendment request: November 7, 1996.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 4.2.9, Service and Instrument Air 
    System, to add an additional air compressor.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change does not:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Utilizing the existing piping configuration, both the new and 
    the existing air compressors are capable of supporting either 
    portion of the Service and Instrument Air System. The addition of 
    the fourth air compressor will decrease the probability of an 
    accident previously evaluated, because capacity is being added to 
    the system. The consequences of an accident previously evaluated 
    will not be affected by the addition of a fourth air compressor. The 
    Service and Instrument Air System performs the non-safety related 
    function of providing compressed air for service use and moisture 
    free compressed instrument air for control air demands. The 
    instrument air portion is designed so that its operation is required 
    for plant reliability, not plant nuclear safety. Safety-related 
    equipment supplied by instrument air is designed to fail in its safe 
    condition upon loss of instrument air or, safety-related equipment 
    (and nonsafety-related equipment determined to be important to 
    safety) required to operate subsequent to instrument air failure is 
    supplied by backup nitrogen accumulators.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The operation of the equipment in the Service and Instrument Air 
    System is essentially unchanged. The new air compressor is a similar 
    design (nonlubricated), providing additional air volume at a quality 
    comparable to the three existing air compressors. Therefore, the 
    possibility of an accident of a different kind than any previously 
    evaluated has not been created.
        (3) Involve a significant reduction in a margin of safety
        The Technical Specification does not specify a margin of safety 
    for the operation of the Service and Instrument Air System, other 
    than specifying that [``Instrument and service] air shall be 
    supplied by three, nonlubricated air compressors, each rated at 70 
    scfm [standard cubic feet per minute]. Instrument air shall also 
    pass through a dryer.'' Addition of a fourth air compressor will 
    increase the available capacity, thus increasing the margin of 
    safety. Therefore, adding the statement ``and one, nonlubricated air 
    compressor rated at 100 scfm'' to Technical Specification 4.2.9. 
    will not reduce the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: John N. Hannon.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of amendment request: October 4, 1996.
        Description of amendment request: The proposed amendment would 
    revise the surveillance requirements in Technical Specifications (TSs) 
    4.1.2.3.1, 4.1.2.4.1, 4.5.2.b, and 4.6.2.1.b and associated Bases. The 
    subject surveillance requirements are applicable to the charging/high 
    head safety injection pumps, low head safety injection pump, and the 
    containment quench spray pumps. The proposed changes would replace the 
    current specific test acceptance criteria contained in these 
    surveillance requirements with requirements to verify pump performance 
    in accordance with the Inservice Testing Program, the Emergency Core 
    Cooling System Flow Analysis, or the Containment Integrity Safety 
    Analysis, as applicable. The proposed changes would also make minor 
    editorial changes in these TSs and make conforming changes in the TS 
    Index pages.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The change does not result in a modification to plant equipment 
    nor does it affect the manner in which the plant is operated. Since 
    the physical plant equipment and operating practices are not 
    changed, as noted above, there is no change in the probability of an 
    accident previously evaluated.
        The proposed change will not lower the pump performance 
    operability criteria for the charging/high head safety injection, 
    low head safety injection and quench spray pumps, as assumed in the 
    safety analysis. The required values for developed pump head and 
    flow will continue to satisfy accident mitigation requirements and 
    will be maintained and controlled in the Inservice Testing (IST) 
    Programs(s).
        Since the proposed change does not lower the pump's performance 
    acceptance criteria, as assumed in the safety analysis, the 
    containment depressurization system will continue to meet its design 
    basis requirements. The proposed change will not impose additional 
    challenges to the containment structure in terms of peak pressure. 
    The calculated offsite dose consequences of a design basis accident 
    (DBA) will remain unchanged since the one hour release duration and 
    source term remain unchanged. The ability of the emergency core 
    cooling system (ECCS) subsystems to provide sufficient emergency 
    core cooling capability in the event of a loss of coolant accident 
    (LOCA) remains unchanged. Therefore, peak cladding temperatures 
    during a LOCA will continue to remain within acceptable limits. The 
    ability of the ECCS subsystems to provide sufficient long term core 
    cooling capability in the recirculation mode during the accident 
    recovery period remains unchanged. The charging pumps, as part of 
    the boron injection system, will continue to provide sufficient flow 
    to ensure negative reactivity control during each mode of facility 
    operation. Future changes to the pump head and flow requirements 
    will be made under the 10 CFR 50.59 process to ensure that the 
    system performance requirements continue to be met.
        The proposed change to the Bases section will ensure that safety 
    analyses assumptions for assumed pump performance continue to be 
    met. The words ``required developed head'' will be clearly defined 
    to reflect that they refer to the value(s) assumed in the safety 
    analysis for the pump's developed head at a specific or a given 
    point. The proposed changes to the Index pages and the footnote in 
    LCO 3.1.2.4 are administrative in nature and do not affect plant 
    safety.
        Based on the above discussion, it is concluded that this change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not alter the method of operating the 
    plant. The charging pumps will continue to be in service during 
    plant operation and be available to perform their function as high 
    head safety injection pumps. This proposed change does not pose 
    additional challenges to the design or function of the charging 
    pumps. The low head safety injection and quench spray
    
    [[Page 66707]]
    
    systems are accident mitigation systems and are normally in standby. 
    System operation would be initiated as required to mitigate the 
    consequences of a DBA. The charging/high head safety injection, low 
    head safety injection and quench pumps will continue to provide 
    sufficient flow to mitigate the consequences of a DBA. These 
    systems' operation continues [sic] [continue] to fulfill the safety 
    functions for which they were designed and no changes to plant 
    equipment will occur. As a result, an accident which is new or 
    different than any already evaluated in the Updated Final Safety 
    Analysis Report will not be created due to this change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety? The surveillance requirements for demonstrating that the 
    pumps are operable will continue to assure the ability of the system 
    to satisfy its design function. Therefore, the proposed change will 
    not affect the ability of these systems to perform their safety 
    function.
        The containment systems' design requirements to restore the 
    containment to subatmospheric condition within one hour will 
    continue to be satisfied. This proposed change does not have an 
    effect on the containment peak pressure since the charging/high head 
    safety injection, low head safety injection and quench spray pumps' 
    performance requirements are not being lowered. The ability of the 
    ECCS subsystems to provide sufficient emergency core cooling 
    capability in the event of a LOCA remains unchanged. Therefore, peak 
    cladding temperatures during a LOCA will continue to remain within 
    acceptable limits. The ability of the ECCS subsystems to provide 
    sufficient long term core cooling capability in the recirculation 
    mode during the accident recovery period remains unchanged. The 
    charging pumps, as part of the boron injection system, will continue 
    to provide sufficient flow to ensure negative reactivity control 
    during each mode of facility operation. There is no resultant change 
    in dose consequences since source term remains unchanged and the 
    containment will continue to reach a subatmospheric pressure within 
    the first hour following a DBA.
        Each pump's performance requirements will continue to be 
    controlled in a manner to ensure safety analysis assumptions are 
    met.
        Therefore, based on the above discussions, it can be concluded 
    that the proposed change does not involve a significant reduction in 
    a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant Units 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: October 31, 1996.
        Description of amendment request: The proposed amendments will 
    revise administrative controls Technical Specification (TS) 6.5.1, 
    ``Facility Review Group (FRG),'' and TS 6.8, ``Procedures and 
    Programs.'' The revisions to TS 6.5.1 reduce the scope of procedures 
    and procedure changes which require review by the FRG, transfer 
    approval of certain procedures from the Plant Manager to the FRG, and 
    require copies of FRG meeting minutes be provided to the Plant Manager. 
    The changes to TS 6.8 reflect the corresponding changes in TS 6.5.1, 
    and expand the scope of the section on temporary changes to procedures.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
    
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments revise certain administrative controls 
    involved with the on-site programmatic process for review and 
    approval of plant procedures. Specifications that are in place to 
    provide assurance that the unit operating staff qualifications are 
    acceptable, and that written procedures are established, implemented 
    and maintained for safety related activities are not being changed. 
    The revisions are consistent with industry standards established 
    pursuant to 10 CFR Part 50, Appendix B, and do not alter any 
    parameter or equipment performance assumptions that are contained in 
    plant safety analyses to evaluate the initiation or consequences of 
    an accident. Therefore, operation of either facility in accordance 
    with its proposed amendment would not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendments will not change the physical plant or 
    the modes of plant operation defined in the Facility License for 
    either St. Lucie unit. Changes proposed for the administrative 
    controls do not involve the addition or modification of equipment 
    nor do they alter the design or operation of plant systems. 
    Therefore, operation of either facility in accordance with its 
    proposed amendment would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed amendments revise certain administrative controls 
    involving the on-site programmatic process for review and approval 
    of plant procedures. The scope, or the requirement to establish, 
    maintain, and implement procedures for activities that could affect 
    nuclear safety are not being changed. The proposed changes are 
    consistent with approved industry standards and do not alter the 
    basis for any technical specification that is related to the 
    establishment of, or the maintenance of, a nuclear safety margin. 
    Therefore, operation of either facility in accordance with its 
    proposed amendment would not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
        Attorney for licensee: M. S. Ross, Attorney, Florida Power & Light, 
    11770 US Highway 1, North Palm Beach, Fl 33408.
        NRC Project Director: Frederick J. Hebdon.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: October 31, 1996 (TSCR 205).
        Description of amendment request: The proposed change requests 
    deletion of Technical Specification Table 3.5.2 which lists automatic 
    primary containment isolation valves. In addition, this change request 
    clarifies the applicability of an action statement which applies to 
    several limiting conditions for operation in Section 3.5 and deletes 
    closure time requirements for several automatic isolation valves in 
    Section 4.5.F.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    
    [[Page 66708]]
    
    
        1. The proposed deletion of the automatic primary containment 
    isolation valve Table 3.5.2 and closure times for several valves in 
    Specification 4.5.F.1 are administrative in nature and do not affect 
    the purpose, function, operability and testing requirements of the 
    automatic primary containment isolation valves or the isolation 
    condenser isolation valves. The required action contained in 
    Specification 3.5.A.7 has been moved to the associated 
    specifications and has not changed. Capitalizing definitions and 
    deleting unneeded pages are also administrative changes which 
    enhance the usability of the Technical Specifications. Therefore, 
    the proposed changes do not increase the probability of occurrence 
    or consequence of an accident previously evaluated.
        2. The proposed changes are administrative and do not involve a 
    physical change to plant configuration nor do they affect the 
    performance of any equipment. Existing limiting conditions for 
    operation and surveillance requirements are retained. Therefore, the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated is not created.
        3. Deleting the list of valves in Table 3.5.2 and valve closure 
    times in Specification 4.5.F.1 are administrative changes which do 
    not affect the purpose or function of the automatic primary 
    containment isolation valves. The listing of the automatic primary 
    containment isolation valves and stroke time requirements will be in 
    controlled plant procedures. Changes to the list or closure times 
    can be made in accordance with review procedures required by Section 
    6.5 of the Technical Specifications and 10 CFR 50.59. Similarly, 
    inserting the statement of required action in Specification 3.5.A.7 
    into the Specifications to which it applies does not modify the 
    condition or the action to be taken and is an administrative change 
    which clarifies the Technical Specifications. Therefore, the margin 
    of safety is not reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: November 12, 1996, as supplemented 
    November 27, 1996 (TSCR 224).
        Description of amendment request: The proposed technical 
    specification change will reflect the implementation of the revised 10 
    CFR Part 20, ``Standards for Protection Against Radiation.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated.
        The proposed revisions to the liquid release rate limits and 
    bases and gaseous effluent bases will not result in a change in the 
    types or amounts of effluents released nor will there be an increase 
    in individual or cumulative radiation exposures. In addition, these 
    changes do not impact the operation or design of any plant 
    structures, systems, or components. These changes ensure compliance 
    with 10 CFR 50.36a and 10 CFR 50 Appendix I and result in levels of 
    radioactive materials in effluents being maintained ALARA [as low as 
    is reasonably achievable]. The revision to the high radiation area 
    controls and dose measurement distance will ensure areas are 
    conservatively posted as high radiation areas in compliance with 10 
    CFR 20.1601(a)(1) and provide controls to ensure individuals are not 
    overexposed. Other proposed changes consist of revisions to 10 CFR 
    20 references to recognize the new section numbers, and 
    administrative controls for record keeping to maintain compliance 
    with the new Part 20.
        These changes will not result in a change to plant design or 
    operation. Therefore, it can be concluded that the proposed changes 
    do not involve an increase in the probability or consequences of an 
    accident previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The 
    proposed changes do not affect the plant design or operation nor do 
    they result in a change to the configuration of any equipment. There 
    will be no change in the types or increase in the amount of 
    effluents released offsite.
        Therefore, this proposed change cannot create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed revisions do not involve any change in the types or 
    increase in the amount of effluents released offsite. The proposed 
    changes do not involve any actual change in the methodology used in 
    the control of radioactive wastes or radiological environmental 
    monitoring. The methodology that will be used in the control of 
    radioactive effluents and calculation of effluent monitor setpoints 
    will result in the same effluent release rate as the current 
    methodology now being used. The operational flexibility needed for 
    releases allows the use of limits as proposed. In addition, the 
    changes in measurement distances for determination of high radiation 
    areas will not result in an increase in individual or cumulative 
    occupational radiation exposures since it will result in a more 
    conservative identification of high radiation areas. Compliance with 
    the limits of the new 10 CFR 20.1301 will be demonstrated by 
    operating within the limits of 10 CFR 50 Appendix I and 40 CFR 190. 
    Thus, operation of the facility in accordance with the proposed 
    amendment does not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: August 29, 1996, as supplemented October 
    3, 1996. The October 3, 1996, submittal contained editorial changes 
    only and did not change the initial no significant hazards 
    consideration evaluation.
        Description of amendment request: The purpose of this amendment 
    request is to incorporate certain improvements from the Standard 
    Technical Specifications for B&W Plants, NUREG-1430.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
        GPU Nuclear has determined that this Technical Specification Change 
    Request involves no significant hazards consideration as defined in 10 
    CFR 50.92 because:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the
    
    [[Page 66709]]
    
    consequences of an accident previously evaluated. The proposed 
    amendment deletes limiting conditions for operation (LCOs) from the 
    TMI-1 Technical Specifications that are no longer required to be 
    addressed in Technical Specifications per 10 CFR 50.36(c)(2)(ii). 
    The proposed amendment deletes Surveillance Requirements from the 
    TMI-1 Technical Specifications that are related to the LCOs to be 
    deleted. These items are addressed in licensee controlled documents. 
    Certain design feature specifications are also to be deleted 
    consistent with the RSTS [Revised Standard Technical Specifications] 
    for B&W plants. The proposed changes do not modify the operation, 
    limits or controls of systems, structures or components relied upon 
    to prevent or mitigate the consequences or accidents previously 
    evaluated.
        Also, the reliability of systems and components relied upon to 
    prevent or mitigate the consequences of accidents previously 
    evaluated is not degraded by the proposed changes. Therefore, this 
    change does not involve a significant increase in the probability of 
    occurrence or the consequences of an accident previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated because no 
    new failure modes are created by the proposed changes.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety because the proposed amendment does not change any operating 
    limits for reactor operation.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: September 20, 1996.
        Description of amendment request: The proposed amendment would 
    revise the Nine Mile Point Unit 1 (NMP1) Technical Specifications that 
    involve the frequencies of surveillance requirements stated in Tables 
    4.6.2a, 4.6.2b, 4.6.2g, and 4.6.11, and Sections 4.2.5b(1), 4.3.2b, 
    4.3.6b(1), 4.3.6b(2), 4.3.6b(3), 4.3.6b(4), 4.3.6c(2), 4.6.13b.1, and 
    4.6.13b.2. The surveillances associated with these tables and sections 
    are currently satisfied during NMP1 refueling outages prior to restart 
    of the unit. The proposed changes would permit surveillance testing 
    either while the reactor is operating or during outage periods not 
    associated with refueling. The requirements of the surveillance 
    sections and tables addressed by this request that are not changed to 
    be performed at power are being changed to allow surveillance credit to 
    be taken for performance of the associated surveillances while the 
    plant is in the Cold Shutdown, Refueling, or Major Maintenance modes. 
    In addition to these proposed changes, typographical errors are 
    corrected.
        Basis for proposed no significant hazards consideration 
    determination: The licensee states that: ``The periods between 
    surveillances will not be inappropriately lengthened. For the affected 
    surveillances, NMP1 administrative controls will require that the 
    interval between surveillance testing not exceed a period equal to 1.25 
    times the nominal 24 months frequency (no longer than 30 months). The 
    NMP1 plant preventive maintenance and surveillance database will be 
    revised accordingly.''
        The licensee groups the systems affected by this request into four 
    categories:
    
        Category 1: The associated system will remain operable and able 
    to automatically perform its safety function during performance of 
    surveillances that satisfy the proposed surveillance requirement.
        Category 2: The system is required for monitoring purposes only 
    and provides no automatic safety actuation function and redundant, 
    or redundant and alternate channels are available for required 
    monitoring.
        Category 3: There is no change in the system configuration or 
    plant operating conditions during the performance of associated 
    surveillances whether the plant is shutdown for refueling or 
    shutdown for maintenance. The surveillances performed to meet the 
    requirements of NMP1 Technical Specifications Tables 4.6.2a 
    Parameter 8 and 4.6.2g Parameter 6 are included in this category and 
    may also be completed in concurrence with a unit shutdown. The only 
    difference between the proposed changes and the normal unit shutdown 
    sequence is that the mode switch may be taken to ``Shutdown'' in 
    order to scram the plant. The response of the plant is the same as 
    it is under the current plant shutdown procedures. There are no 
    other differences in testing techniques or testing criteria from 
    those previously required by the NMP1 Technical Specifications.
        Category 4: The system or equipment is isolated or out of 
    service during the performance of the required surveillances. The 
    associated surveillance may be performed concurrently with quarterly 
    valve stroking, at which time the system or equipment is already out 
    of service.
    
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequence of an accident previously evaluated.
        Each of the four categories [* * *] are evaluated separately below:
    
        Category 1: The associated systems will remain operable and able 
    to automatically fulfill as designed any required safety functions 
    that may become necessary during performance of required 
    surveillances. No physical change to the plant design, materials, or 
    standards is involved. No change to instrumentation operating 
    characteristics outside current tolerances will be made. No plant 
    transients will be initiated as a result of the proposed changes. No 
    initiator of any accident previously evaluated is adversely 
    affected. No system required to actuate to respond to any accident 
    previously evaluated in the UFSAR [Updated Final Safety Analysis 
    Report] is adversely affected by the proposed change.
        Category 2: The associated systems will be required for 
    monitoring purposes only and provide no automatic safety actuation 
    function and redundant, or redundant and alternate channels are 
    available for required monitoring. Since redundant monitoring 
    instrumentation will still be available as required by the technical 
    specifications, the associated systems' functions in accident 
    mitigation are not affected. No physical change to the plant design, 
    materials, or standards is involved. No change to instrumentation 
    operating characteristics outside current tolerances will be made. 
    No plant transients will be initiated as a result of the proposed 
    changes. No initiator of any accident previously evaluated is 
    adversely affected. No system required to actuate to respond to any 
    accident previously evaluated in the UFSAR is adversely affected by 
    the proposed changes.
        Category 3: There will be no change in the system configuration 
    or plant operating conditions during the performance of associated 
    surveillances. The associated system's ability to perform required 
    safety functions will not be affected, whether the plant is shutdown 
    for refueling or shutdown for maintenance. The surveillances 
    performed to meet the requirements of NMP1 Technical Specifications 
    Tables 4.6.2a Parameter B and 4.6.2g Parameter 6 are included in 
    this category and may also be performed in concurrence with a unit 
    shutdown. The only difference between the proposed changes and the 
    normal unit shutdown sequence is that the mode switch
    
    [[Page 66710]]
    
    may be taken to ``Shutdown'' in order to scram the plant. The 
    response of the plant is the same as it is under the current plant 
    shutdown procedures. There are no other differences in testing 
    techniques or testing criteria from those previously required by the 
    NMP1 Technical Specifications. No physical change to the plant 
    design, materials, or standards is involved. No change to 
    instrumentation operating characteristics outside current tolerances 
    will be made. No unexpected plant transients will be initiated as a 
    result of the proposed changes. No initiator of any accident 
    previously evaluated is adversely affected. No system required to 
    actuate to respond to any accident previously evaluated in the UFSAR 
    is adversely affected by the proposed changes.
        Category 4: The associated system or equipment will be isolated 
    or out of service during the performance of the required 
    surveillances. The associated surveillances will be performed during 
    quarterly valve stroking, at which time the system or equipment is 
    already out of service. No physical change to the plant design, 
    materials, or standards is involved. No change to instrumentation 
    operating characteristics outside current tolerances will be made. 
    No plant transients will be initiated as a result of the proposed 
    changes. No initiator of any accident previously evaluated is 
    adversely affected. No system required to actuate to respond to any 
    accident previously evaluated in the UFSAR is adversely affected by 
    the proposed changes.
    
        The correction of the typographical errors is administrative only 
    and has no affect on plant systems or procedures. In all cases, 
    equipment used for accident mitigation is not adversely affected. The 
    ability of the operators to safely shut down NMP1 is not impaired. The 
    changes will not adversely affect any accident precursor or initiator 
    of any accident. For these reasons, the proposed changes will not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Each of the four categories [* * *] are evaluated separately below.
    
        Category 1: The associated systems will remain operable and able 
    to automatically perform as designed any required safety functions 
    that may become necessary during performance of required 
    surveillances. No physical change to the plant design, materials, or 
    standards is involved. No change to instrumentation operating 
    characteristics outside current tolerances will be made. No accident 
    initiator or failure of a different type than previously identified 
    in the UFSAR is introduced. No different or new plant transients may 
    result from those previously evaluated in the UFSAR.
        Category 2: The associated systems will be required for 
    monitoring purposes only and provide no automatic safety actuation 
    function. Since redundant, or redundant and alternate monitoring 
    instrumentation will still be available as required by the technical 
    specifications, the associated systems' functions in accident 
    mitigation are not affected. No physical change to the plant design, 
    materials, or standards is involved. No change to instrumentation 
    operating characteristics outside current tolerances will be made. 
    No accident initiator or failure of a different type than previously 
    identified in the UFSAR is introduced. No different or new plant 
    transients may result from those previously evaluated in the UFSAR.
        Category 3: There will be no change in the system configuration 
    or plant operating conditions during the performance of associated 
    surveillances. The associated system's ability to perform required 
    safety functions will not be affected, whether the plant is shutdown 
    for refueling or shutdown for maintenance. The surveillances 
    performed to meet the requirements of NMP1 Technical Specifications 
    Tables 4.6.2a Parameter 8 and 4.6.2g Parameter 6 are included in 
    this category and may also be performed in concurrence with a unit 
    shutdown. The only difference between the proposed changes and the 
    normal unit shutdown sequence is that the mode switch may be taken 
    to ``Shutdown'' in order to scram the plant. The response of the 
    plant is the same as it is under the current plant shutdown 
    procedures. There are no other differences in testing techniques or 
    testing criteria from those previously required by the NMP1 
    Technical Specifications. No physical change to the plant design, 
    materials, or standards is involved. No change to instrumentation 
    operating characteristics outside current tolerances will be made. 
    No unexpected plant transients will be initiated as a result of the 
    proposed changes. No accident initiator or failure of a different 
    type than previously identified in the UFSAR is introduced. No 
    different or new plant transients may result from those previously 
    evaluated in the UFSAR.
        Category 4: The associated system or equipment will be isolated 
    or out of service during the performance of the required 
    surveillance. The associated surveillances will be performed during 
    quarterly valve stroking, at which time the system or equipment is 
    already out of service. No physical change to the plant design, 
    materials, or standards is involved. No change to instrumentation 
    operating characteristics outside current tolerances will be made. 
    No plant transients will be initiated as a result of the proposed 
    changes. No accident initiator or failure of a different type than 
    previously identified in the UFSAR is introduced. No different or 
    new plant transients may result from those previously evaluated in 
    the UFSAR.
    
        The correction of the typographical errors is administrative only 
    and has no affect on plant systems or procedures. In all cases, the 
    changes will not adversely affect any accident precursor or initiator 
    of any accident and, therefore, the changes do not introduce any new 
    failure modes or conditions that may create a new or different 
    accident. For these reasons, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated in the UFSAR.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        Each of the four categories [* * *] are evaluated separately below.
    
        Category 1: The associated systems will remain operable and able 
    to automatically perform required safety functions during 
    performance of surveillances that satisfy the surveillance 
    requirement. There will be no effective change in the interval of 
    the affected surveillances. The probability of instrument drift or 
    the ability to detect a failed or drifted instrument remains 
    unchanged. No physical change to the plant design, materials, or 
    standards is involved. No change to instrumentation operating 
    characteristics outside current tolerances will be made. No system 
    required to actuate to respond to any accident is adversely affected 
    by the proposed changes. Since each system's operability is not 
    affected, the margin of safety associated with these systems will 
    not be significantly reduced.
        Category 2: The associated systems will be required for 
    monitoring purposes only and provide no automatic safety actuation 
    function. Redundant, or redundant and alternate monitoring 
    instrumentation will still be available as required by the technical 
    specifications during the performance of the associated 
    surveillances. No physical change to the plant design, materials, or 
    standards is involved. No change to instrumentation operating 
    characteristics outside current tolerances will be made. There will 
    be no effective change in the intervals of the affected 
    surveillances. The probability of instrument drift or the ability to 
    detect a failed or drifted instrument remains unchanged. No plant 
    transients will be initiated as a result of the proposed changes. No 
    initiator of any accident previously evaluated is adversely 
    affected. No system required to actuate to respond to any accident 
    is adversely affected by the proposed changes. Therefore, the 
    associated systems' functions in accident mitigation are not 
    affected, and no margin of safety will be significantly reduced.
        Category 3: There will be no change in the system configuration 
    or plant operating conditions during the performance of associated 
    surveillances, the associated system's ability to perform required 
    safety functions will not be affected, whether the plant is shutdown 
    for refueling or shutdown for maintenance. The surveillances 
    performed to meet the requirements of NMP1 Technical Specifications 
    Tables 4.6.2a Parameter 8 and 4.6.2g Parameter 6 may also be 
    completed in concurrence with a unit shutdown. The only difference 
    between the proposed changes and the normal unit shutdown sequence 
    is that the mode switch may be taken to ``Shutdown'' in order to
    
    [[Page 66711]]
    
    scram the plant. The response of the plant is the same as it is 
    under the current plant shutdown procedures. There are no other 
    differences in testing techniques or testing criteria from those 
    previously required by the NMP1 Technical Specifications. No 
    physical change to the plant design, materials, or standards is 
    involved. No change to instrumentation operating characteristics 
    outside current tolerances will be made. There will be no effective 
    change in the intervals of the affected surveillances. The 
    probability of instrument drift or the ability to detect a failed or 
    drifted instrument remains unchanged. No unexpected plant transients 
    will be initiated as a result of the proposed changes. No initiator 
    of any accident if adversely affected. No system required to actuate 
    to respond to any accident previously evaluated is adversely 
    affected by the proposed changes. Therefore, no margin of safety 
    will be significantly reduced.
        Category 4: The associated system or equipment will be isolated 
    or out of service during the performance of the required 
    surveillances. The associated surveillances will be performed during 
    quarterly valve stroking, at which time the system or equipment will 
    already be out of service. No physical change to the plant design, 
    materials, or standards is involved. No change to instrumentation 
    operating characteristics outside current tolerances will be made. 
    There will be no effective change in the intervals of the affected 
    surveillances. The probability of instrument drift or the ability to 
    detect a failed or drifted instrument remains unchanged. No plant 
    transients will be initiated as a result of the proposed changes. No 
    accident initiator or failure of a different type than identified in 
    the UFSAR is introduced. Therefore, no margin of safety will be 
    significantly reduced.
    
        The correction of the typographical errors is administrative only 
    and has no affect on plant systems or procedures. In all cases, the 
    changes will not adversely affect any accident precursor or initiator 
    of any accident and, therefore, the changes do not introduce any new 
    failure modes or conditions that may create a new or different 
    accident. None of the proposed changes involve physical modification of 
    the plant or alterations to any accident or transient analysis. 
    Therefore, for this and the above reasons, these proposed changes do 
    not involve any significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa, Acting Director.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: October 16, 1996.
        Description of amendment request: The proposed amendment would 
    change certain requirements stated in Technical Specification 3/4.8.1, 
    ``AC Sources''. The requirements are related to the emergency diesel 
    generators (EDGs). The proposed changes would:
        1. Increase the EDG fuel storage system minimum volume requirements 
    specified in Limiting Condition for Operation 3.8.1.1.b.2;
        2. Add a footnote applicable to Surveillance Requirement 
    4.8.1.1.2.f to qualify the words during shutdown. The footnote would 
    allow the option of performing selected surveillances, or portions 
    thereof, during conditions or modes other than shutdown;
        3. Delete from Surveillance Requirement 4.8.1.1.2.f.14 the 
    requirement to verify that the cooling tower fans start automatically 
    on a Tower Actuation signal; and
        4. Delete Surveillance Requirement 4.8.1.1.2.h.2 which specifies 
    performing a periodic pressure test on the ASME Code Class 3 diesel 
    fuel oil piping.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 CFR 
    50.92(c)(1)).
    1. Limiting Condition for Operation  3.8.1.1.b.2
        The proposed change increases the minimum EDG fuel oil storage 
    requirement to account for various factors that may affect the fuel 
    consumption rate. The revised storage requirement reflects actual EDG 
    test data and accounts for external variables including fuel oil 
    specific gravity, heating value of the fuel, and ambient conditions. 
    The proposed increase in the minimum volume storage requirement is 
    conservative and ensures that there will be at least a 7 day supply of 
    fuel oil stored for each EDG to meet the maximum Engineered Safety 
    Feature load requirements following a loss of power and a design basis 
    accident as described in Updated Final Safety Analysis Report (UFSAR) 
    Section 9.5.4.1, Diesel Generator Fuel Oil Storage and Transfer 
    System--Design Basis. Therefore, the proposed change does not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
    2. Surveillance Requirement  4.8.1.1.2.f
        The proposed change qualifies the requirement to perform EDG 
    surveillance requirements ``during shutdown''. Because the terms Hot 
    Shutdown and Cold Shutdown are defined in the TSs as operating modes or 
    conditions, the requirement to perform certain surveillances during 
    shutdown may be misinterpreted, as noted in NRC Generic Letter 91-04. 
    The proposed footnote would permit certain maintenance and testing 
    activities to be performed during conditions or modes other than 
    shutdown. The proposed footnote to Surveillance Requirement 4.8.1.1.2.f 
    would not alter the intent or the method by which the surveillances are 
    conducted, and the acceptance criteria for the surveillances would be 
    unchanged. The footnote would not degrade the ability of the EDGs to 
    perform their intended function, and it would not affect the response 
    of the EDGs to a loss of power as described in the UFSAR. Since plant 
    response to an accident would not change and since failure of an EDG 
    could not initiate any of the accidents evaluated in the UFSAR, the 
    proposed footnote would not alter the probability or consequences of an 
    accident previously analyzed.
    3. Surveillance Requirement  4.8.1.1.2.f.14
        The cooling tower functions as the ultimate heat sink following a 
    seismic event which results in blockage of the circulating water 
    tunnels and therefore a loss of service water. Amendment 18 eliminated 
    the requirement for automatic start of the cooling tower fans; 
    therefore, the automatic-start function for the cooling tower fans has 
    been defeated by placing the control switch in ``Pull-to-Lock''. The 
    proposed change to delete the automatic fan start reference from 
    Surveillance Requirement 4.8.1.1.2.f.14 is administrative only to 
    correct an oversight since the requirement should have been deleted 
    with the issuance of Amendment 18. The proposed deletion does not 
    affect the manner by which the facility is operated or involve any
    
    [[Page 66712]]
    
    changes to equipment or features which affect the operational 
    characteristics of the facility. Since there is no change to the 
    facility or operating procedures, there is no affect upon the 
    probability or consequences of any accident previously analyzed.
    4. Surveillance Requirement  4.8.1.1.2.h.2
        The ASME Code, Section XI, including applicable ASME Code Cases as 
    authorized by the NRC, provides alternate test methods to use in lieu 
    of a 110% hydrostatic pressure test that is not practical to perform on 
    the EDG fuel oil system as currently designed. With the proposed 
    deletion of Surveillance Requirement 4.8.1.1.2.h.2, the provisions of 
    Surveillance Requirement 4.0.5 and the ASME Code along with NRC-
    authorized Code Cases would be utilized as an equivalent testing 
    requirement to ensure the continued integrity of the diesel fuel oil 
    system. Therefore, since the reliability of the EDG fuel oil system 
    will not be reduced, the probability or consequences of any accident 
    previously evaluated is not increased.
        B. The changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)).
    1. Limiting Condition for Operation 3.8.1.1.b.2
        The proposed minimum fuel storage requirement has been developed 
    using actual EDG performance data and accounting for possible 
    variations in fuel oil specific gravity, heating value of the fuel, and 
    ambient conditions. The proposed change will provide additional 
    assurance that there will be at least a 7 day supply of fuel oil to 
    meet the maximum Engineered Safety Feature load requirements following 
    a loss of power and a design basis accident. The amount of fuel oil 
    stored has no effect upon the initiation of any accident sequence, 
    therefore, the proposed change does not create the possibility of a new 
    or different kind of accident from any previously analyzed.
    2. Surveillance Requirement 4.8.1.1.2.f
        The proposed change to allow the option (as supported by a 10 CFR 
    50.59 safety evaluation) of performing selected surveillance tests, or 
    portions thereof, during conditions or modes other than during shutdown 
    does not affect the operation or response of any plant equipment, 
    including the EDGs, or introduce any new failure mechanism. Therefore, 
    the proposed change does not create the possibility of a new or 
    different kind of accident from any previously analyzed.
    3. Surveillance Requirement 4.8.1.1.2.f.14
        Amendment 18 to the Seabrook Station Operating License approved the 
    change in the cooling tower operating mode from automatic actuation to 
    manual actuation. The proposed change to Surveillance Requirement 
    4.8.1.1.2.f.14 does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because it does not affect the manner by which the 
    facility has been operated since Amendment 18 was issued, involve any 
    changes to equipment or features which affect the operational 
    characteristics of the facility, or introduce a new failure mode. The 
    proposed change merely corrects an oversight in that the requirement 
    should have been deleted when Amendment 18 was issued.
    4. Surveillance Requirement 4.8.1.1.2.h.2
        The change does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because it does not affect the manner by which the 
    facility is operated as assumed in the design analysis or Safety 
    Evaluation, involve any changes to equipment or features which affect 
    the operational characteristics of the facility, or introduce a new 
    failure mode. The proposed change merely provides a practical alternate 
    test method using methods acceptable per Section XI of the ASME Code, 
    applicable ASME Code Cases as authorized by the NRC, and Regulatory 
    Guide (RG) 1.137, ``Fuel-Oil Systems at Nuclear Power Plants,'' 
    Revision 1, October 1979. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from any 
    previously analyzed.
        C. The changes do not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)).
    1. Limiting Condition for Operation 3.8.1.1.b.2
        The proposed change does not reduce the ability of the EDGs to 
    provide sufficient power for at least 7 days to meet the maximum 
    Engineered Safety Feature load requirements following a loss of power 
    and a design basis accident as described in UFSAR Section 9.5.4.1.
    2. Surveillance Requirement 4.8.1.1.2.f
        The proposed change does not reduce the ability of the EDGs to 
    provide sufficient power to meet the maximum Engineered Safety Feature 
    load requirements following a loss of power and a design basis accident 
    as described in the UFSAR. Performing certain surveillances during 
    conditions or modes other than shutdown (as supported by a 10 CFR 50.59 
    safety evaluation) does not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)) because it does not affect the manner by 
    which the facility is operated as assumed in the design analysis or 
    Safety Evaluation, involve any changes to equipment or features which 
    affect the operational characteristics of the facility. The proposed 
    change will continue to ensure the reliability of the EDGs to perform 
    their intended function.
    3. Surveillance Requirement  4.8.1.1.2.f.14
        The change does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because it does not affect the manner by which the 
    facility has operated since Amendment 18 was issued, involve any 
    changes to equipment or features which affect the operational 
    characteristics of the facility, or introduce a new failure mode. The 
    proposed change merely corrects an oversight in that the requirement 
    should have been deleted when Amendment 18 was issued.
    4. Surveillance Requirement  4.8.1.1.2.h.2
        The change does not involve a significant reduction in a margin of 
    safety (10 CFR 50.92(c)(3)) because it does not affect the manner by 
    which the facility is operated or involve any changes to equipment or 
    features which affect the operational characteristics of the facility. 
    The proposed change will continue to ensure the reliability of the EDG 
    fuel oil system. The proposed change merely provides a practical 
    alternate test method using methods acceptable per Section XI of the 
    ASME Code, applicable ASME Code Cases as authorized by the NRC, and 
    Regulatory Guide (RG) 1.137, ``Fuel-Oil Systems at Nuclear Power 
    Plants,'' Revision 1, October 1979.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
        Attorney for licensee: Lillian M. Cuoco, Esquire, Northeast 
    Utilities
    
    [[Page 66713]]
    
    Service Company, Post Office Box 270, Hartford CT 06141-0270.
        NRC Project Director: S. Singh Bajwa, Acting.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: October 17, 1996.
        Description of amendment request: The proposed amendment would 
    delete certain instrumentation requirements stated in Technical 
    Specification (TS) 3/4.3, Instrumentation. The deleted requirements 
    would be relocated to the Seabrook Station Technical Requirements 
    Manual (SSTR). The associated Bases for the deleted TS requirements 
    will be deleted also, but they will not be incorporated into the SSTR. 
    The following Limiting Conditions for Operation (LCO) and associated 
    Surveillance Requirements (SRs) would be relocated to the SSTR:
    
    ------------------------------------------------------------------------
             Technical  specification                       Title           
    ------------------------------------------------------------------------
    LCO--3.3.3.2..............................  Incore Detector System.     
    LCO--3.3.3.3 and associated SRs & Tables..  Seismic Instrumentation.    
    LCO--3.3.3.4 and associated SRs & Tables..  Meteorological              
                                                 Instrumentation            
    LCO--3.3.4 and associated SRs.............  Turbine Overspeed           
                                                 Protection.                
    ------------------------------------------------------------------------
    
        The proposed amendment would also delete (without relocating to the 
    SSTR) the reference to the location of the meteorological tower from TS 
    5.5.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 CFR 
    50.92(c)(1)) because the proposed changes do not involve any physical 
    changes to the plant, do not alter the way any structure, system or 
    component functions, do not modify the manner in which the plant is 
    operated, do not impact the physical protective boundaries of the 
    plant, and do not decrease the effectiveness of administrative controls 
    for assuring safe operation of the facility. The instrumentation-
    related systems are not considered a design feature or an operating 
    restriction that is an initial condition of a design basis accident or 
    transient analysis, nor do they function in any way to mitigate the 
    consequences of a design basis accident or transient.
        B. The changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because the proposed changes do not involve any physical 
    changes to the plant, do not alter the way any structure, system or 
    component functions, do not modify the manner in which the plant is 
    operated, do not impact the physical protective boundaries of the 
    plant, and do not decrease the effectiveness of administrative controls 
    for assuring safe operation of the facility.
        C. The changes do not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)) because the proposed changes do not 
    involve any physical changes to the plant, do not alter the way any 
    structure, system or component functions, do not modify the manner in 
    which the plant is operated, do not impact the physical protective 
    boundaries of the plant, and do not decrease the effectiveness of 
    administrative controls for assuring safe operation of the facility. 
    Further, the proposed changes do not affect the ability of systems, 
    structures or components important to safety to perform their intended 
    function.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
        Attorney for licensee: Lillian M. Cuoco, Esquire, Northeast 
    Utilities Service Company, Post Office Box 270, Hartford CT 06141-0270.
        NRC Project Director: S. Singh Bajwa, Acting.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: March 20, 1996 and as supplemented on 
    July 25, 1996.
        Description of amendment request: The amendments would modify the 
    Susquehanna Steam Electric Station (SSES), Units 1 and 2, Technical 
    Specifications to change the ``open'' logic for the high pressure core 
    injection (HPCI) suction valves HV-155/255-F042 in order to eliminate 
    the HPCI pump auto-transfer on high suppression pool level.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Based on the following discussion for the containment, reactor 
    building, HPCI and RCIC [reactor core isolation cooling] systems, 
    and the safety-related valves in piping connected to the suppression 
    pool, the proposed action does not increase the probability or 
    consequences of an accident previously evaluated. Primary 
    Containment and Reactor Building Safety-Related Systems, Structures, 
    and Components Affected by LOCA/SRV [Loss-of-coolant-accident/safety 
    relief valve] Hydrodynamic Loads
        As discussed in the Safety Assessment for this change, 
    elimination of the HPCI auto suction transfer on high suppression 
    pool level will allow higher suppression pool water levels in 
    accidents and transients which involve HPCI operation. The impact of 
    the higher suppression pool levels were examined for the following 
    design-basis accidents and transients:
        Loss of Coolant Accidents inside containment (FSAR [Final Safety 
    Analysis Report] *6.2.1.1.3.3),
        Inadvertent Safety/Relief valve opening (FSAR *15.1.4),
        Primary system break outside containment (FSAR *3.6A),
        Inadvertent HPCI initiation (FSAR *15.5.1),
        Loss of feedwater flow (FSAR *15.2.7),
        Loss of Offsite AC Power (FSAR *15.2.6),
        Loss of Main Condenser vacuum (FSAR *15.2.5),
        Inadvertent MSIV closure (FSAR *15.2.4),
        Turbine trip (with and without bypass) (FSAR *15.2.3),
        Generator Load Rejection (with and without bypass), (FSAR 
    *15.2.2), and
        Pressure regulator failure-closed/open (FSAR *15.2.1 & 15.1.3).
        These accidents and transients were selected for evaluation 
    because they involve an initiation of the HPCI system either 
    inadvertently or as a result of a decrease in vessel inventory and/
    or coolant level. Two special events, ATWS and SBO, are also 
    considered along with the design basis events listed above.
        It was concluded that design-basis SRV and LOCA loads envelop 
    the loads expected with the proposed change. Therefore, the proposed 
    change does not increase the failure probability of any primary 
    containment or reactor building structure, system or component which 
    is affected by LOCA/SRV hydrodynamic loads. The major findings which 
    lead to this conclusion about SRV and LOCA loads are summarized 
    below:
        DBA [design basis accident] dynamic pressure loads are based on 
    a maximum initial suppression pool level of 24 feet. The proposed 
    modification to the HPCI suction
    
    [[Page 66714]]
    
    transfer logic does not affect the initial pool level or the initial 
    suppression chamber air space volume. During normal plant operation, 
    suppression pool level (and hence suppression chamber air space 
    volume) is controlled by Technical Specification requirements.
        For LOCAs other than the DBA, the containment is designed for 
    ADS [automatic depressurization system] blowdown loads in 
    combination with the LOCA loads. For an intermediate break, the 
    proposed HPCI modification does allow suppression pool level to 
    exceed 24 feet by a small amount. ADS loads are, however, 
    independent of suppression pool level when the downcomer vents are 
    cleared. Therefore, the proposed modification has no influence on 
    ADS hydrodynamic loads for an intermediate break.
        For small breaks, HPCI injection prevents ADS actuation. 
    Nevertheless, SRV actuations occur during the RPV [reactor pressure 
    vessel] cooldown. Downcomer vents are opened in the beginning part 
    of the accident, but close later on as the break enthalpy decreases. 
    When the downcomer vents are cleared, the level inside the SRV 
    tailpipe is not influenced by pool level, and therefore, the SRV 
    hydrodynamic loads are unaffected by the proposed modification. 
    During the phase of the accident in which the downcomer vents are 
    sealed with water, there are no wetwell LOCA hydrodynamic loads, but 
    the SRV loads are dependent on SP [suppression pool] water level. In 
    this case, SRV loads are acceptable because SP water level is always 
    below the Load Limit curve.
        ADS actuation would be required in the event of a HPCI failure 
    during a small-break accident. If HPCI fails during the phase of the 
    accident in which the downcomer vents are cleared, then ADS loads 
    would be acceptable because water level (and air volume) within the 
    SRV tailpipes is independent of pool level. Even if HPCI failure 
    occurs in the latter part of the accident where the downcomer vents 
    are sealed, ADS loads are acceptable because water level is always 
    well below the Load Limit curve.
        Under non-LOCA conditions, the containment is designed for 
    simultaneous actuation of all 16 SRVs. The Load Limit Line defines 
    the acceptable operating region, in terms of reactor pressure and 
    suppression pool level, for actuation of all 16 SRVs. Following a 
    plant transient involving HPCI operation, the suppression pool level 
    is always below the Load Limit curve, and only a small number of 
    SRVs actuate to remove decay heat from the reactor.
    
    HPCI System
    
        The proposed change does not increase the probability of an 
    equipment malfunction in the HPCI system. In fact, the change 
    eliminates the potential failure of the HPCI suction auto-transfer 
    on high suppression pool level since that logic is removed. 
    Potential spurious auto-transfer associated with high suppression 
    pool logic is also eliminated. HPCI suction auto-transfer on low CST 
    [condensate storage tank] level and its potential to fail are 
    unchanged by this change. Also, the change does not affect the 
    manual suction transfer from the CST to the suppression pool.
        As discussed in the safety assessment for this change, the 
    proposed change has no adverse effects on HPCI valves, pump, or 
    turbine. Therefore, elimination of the HPCI suction auto transfer 
    logic (on high suppression pool level) does not increase the 
    probability of a HPCI malfunction. The consequence of a HPCI failure 
    in a design-basis accident is evaluated in NEDC-32071P Rev.1, 
    ``Susquehanna Steam Electric Station Units 1 and 2 SAFER/GESTR-LOCA 
    Loss-of-Coolant Accident Analysis.'' With regard to the fuel, the 
    consequence of a HPCI failure is unaffected by the proposed change.
        If HPCI fails in a design-basis small break accident, ADS 
    actuation would be required. ADS loads continue to be enveloped by 
    design loads with the proposed change. Therefore, the proposed 
    change does not increase the consequences of a HPCI failure.
        HPCI Relay Panel 1C620(2C620) & 250 V DC Control Center 
    1D264(2D264)
        On a component level, the failure probability and consequences 
    of failure associated with the AX [auxiliary] relay in 250 VDC 
    Control Center 1D264 (2D264) are eliminated because the relay is 
    disconnected and removed by this modification. Since the control 
    functions of K19 in panel 1C620 (2C620) have been eliminated, the 
    failure of the relay has no effect on HPCI suction valve F042 
    operation.
        The 250 VDC Control Center 1D264 (2D264) and HPCI Relay Panel 
    1C620 (2C620) both receive power from battery systems during Station 
    Blackout. Removal of the relay from 250 VDC Control Center 1D264 
    (2D264) and the replacement of the relay in HPCI Relay Panel 1C620 
    (2C620) decreases the load on the battery systems by a small amount. 
    The change in battery load and line voltage drop is negligible and 
    is documented in applicable calculations. Dynamic qualification of 
    the subject equipment is not adversely affected by this modification 
    as documented in applicable calculations.
    
    RCIC Turbine
    
        As discussed in the safety assessment for this change, RCIC is 
    used to provide coolant makeup following a reactor vessel isolation 
    and for an Appendix R shutdown scenario. The Appendix R event also 
    assumes the reactor vessel is isolated. These events are discussed 
    in Section 15.2.4 of the FSAR and in the FPRR [fire protection 
    review report]. The proposed change has no adverse effects on RCIC 
    turbine operation following a MSIV [main steam isolation valve] 
    closure (see discussion in the safety assessment for this change 
    [letter dated March 20, 1996, as supplemented July 25, 1996]). 
    Therefore, there is no increase in the RCIC failure probability for 
    the MSIV-closure event or the Appendix R shutdown scenario. The 
    consequence of RCIC failure is unchanged by the proposed 
    modification; if RCIC fails, HPCI is available as a backup 
    system.\1\ [All footnotes are listed at the end of the no signficant 
    hazards basis section.]
        Although RCIC is not designed for mitigation of a small break 
    accident, the effect of the proposed change on RCIC turbine 
    operation for such an accident was evaluated in the safety 
    assessment for this change. The assessment concludes that the 
    proposed change has no adverse effects on RCIC operation, and 
    therefore, there is no increase in RCIC failure probability during a 
    small break accident. Failure of RCIC in a small break accident 
    would require ADS initiation only for a particular break flow which 
    is slightly greater than HPCI injection capability. But ADS 
    initiation has already been considered when evaluating the 
    consequences of HPCI failure during a small break accident.
    
    Safety-Related Valves on Piping Connected to Suppression Chamber
    
        MOVs [motor operated valves]--The proposed change could 
    potentially lead to a maximum suppression pool level of 26 feet in a 
    design-basis accident. This is 2 feet above the maximum design level 
    of 24 feet. As discussed in the safety assessment for this change, 
    this is equivalent to a pressure increase of 0.86 psi at the bottom 
    of the suppression pool. This small pressure increase has negligible 
    effect on valve operation, and therefore, there is no increase in 
    the probability of a failure or malfunction of valves in piping 
    connected to the suppression pool.
        Vacuum Breakers--Allowing suppression pool level to potentially 
    increase to 26 feet in a design-basis accident does not affect the 
    failure probability of downcomer-vent vacuum breakers because the 
    level is well below the vacuum breaker elevation of 42 feet.
        SRVs/Tailpipes--As discussed in the safety assessment for this 
    change, the increased suppression pool level associated with the 
    proposed change does not have any adverse effect on SRV operation or 
    on the structural integrity of the SRV tailpipe.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Based on the following discussion for the containment, reactor 
    building, HPCI and RCIC systems, and the safety-related valves in 
    piping connected to the suppression pool, the proposed action does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The following discussion concerning the impact of the change on 
    the primary containment, the reactor building, the HPCI system, and 
    safety-related valves, provides the basis for this conclusion.
    
    Primary Containment and Reactor Building Safety-Related Systems, 
    Structures, and Components Affected by LOCA/SRV Hydrodynamic Loads
    
        The HPCI suction transfer logic is not necessary to maintain 
    LOCA loads within design limits because these dynamic pressure loads 
    are characterized in terms of the SP level at the initiation of the 
    accident. That is, LOCA blowdown tests were conducted without the 
    removal of water from the suppression chamber section of the test 
    tank.2 The increase in pool level realized during these tests 
    was proto-typical of the pool level increase expected at 
    Susquehanna. Removal of the HPCI suction transfer logic on high pool 
    level does not affect suppression pool level at the initiation of a 
    DBA.3
    
    [[Page 66715]]
    
        In addition, the HPCI suction transfer logic is not necessary to 
    maintain SRV/ADS blowdown loads within design limits. SRV dynamic 
    pressure loads consist of two components: air clearing loads and 
    steam condensation loads. The steam condensation loads are bounded 
    by the more severe air clearing loads which are caused by gas bubble 
    oscillations following the expulsion of noncondensible gas from the 
    SRV tailpipe. Air clearing loads are a function of reactor pressure 
    and water level inside the SRV tailpipe.
        Depending on the break size and location, the downcomer vents 
    may be cleared for the entire time that HPCI is operating, or they 
    may reseal in the latter part of the accident. When the downcomer 
    vents are cleared, the level inside the SRV tailpipe is depressed to 
    the elevation coinciding with the bottom of the downcomer pipes, and 
    it is therefore decoupled from the rising suppression pool level. In 
    this situation SRV air-clearing loads are unaffected by the proposed 
    change.
        When the downcomer vents are sealed with water, the Load Limit 
    line can be used to determine if SRV/ADS loads are enveloped by 
    design loads. For the most limiting event, which is the small break 
    LOCA, the overall safety margin increases as pool level rises during 
    the event. This is because the decrease in reactor pressure more 
    than offsets the adverse effects associated with the rise in pool 
    level.
        Since LOCA and SRV dynamic loads remain bounded by design loads, 
    dynamic loading of primary containment and reactor building 
    structures, systems, and components are unaffected by the proposed 
    change. Therefore, with respect to dynamic loads, the proposed 
    change does not create the possibility for an accident or 
    malfunction of a different type than any evaluated in the SAR 
    [Safety Analysis Report].
    
    HPCI System
    
        There are no new HPCI turbine failure modes introduced by the 
    higher suppression pool levels which can occur with the proposed 
    change. Turbine exhaust pressure remains well below the design limit 
    of 65 psia. In addition, the higher pool level does not create the 
    possibility of water hammer damage to the turbine discharge piping. 
    If the operator fails to control RPV level less than +54'' (single 
    operator error) in the long-term part of the small-break accident 
    when suppression pool level is greater than 25.6 feet, leakage 
    through check valve F049 is such that it will be contained well 
    within the volume of the turbine-discharge-line drain pot. Note that 
    suppression pool level is limited to 26 feet by operator action. 
    Furthermore, suppression pool level can reach 26 feet only for a 
    particular range of small breaks, and for this range of small 
    breaks, suppression pool level would exceed 25.6 feet for only 
    approximately 10 minutes of the accident duration. This corresponds 
    to about 10% of the time that HPCI is operating. Thus it is very 
    unlikely that HPCI would trip with pool level greater than 25.6 
    feet.
        If check valve F049 is failed during the small-break accident 
    (single equipment failure), the turbine exhaust line would become 
    flooded if the HPCI system tripped during the 10 minute interval 
    when suppression pool level greater than 26 feet; however, it is not 
    necessary to postulate an operator error (failure to control RPV 
    level less than +54'') along with the check valve failure. A small 
    break accident with failure of check valve F049 and failure of the 
    operator to control RPV level as required by the EOPs [emergency 
    operating procedures], in a narrow time interval during the long-
    term part of the accident, is beyond the plant design basis.
        A new type of malfunction does not occur even in the beyond-
    design-basis condition where failure of check valve F049 is 
    considered along with failure of the operator to control RPV level 
    less than 54'' in the narrow time interval when pool level is 
    greater than 25.6. With these failures, the turbine exhaust piping 
    will become flooded, and the system may fail on restart. The General 
    Electric Company has performed an analysis to determine the 
    consequences of a HPCI start with flooding of the turbine and 
    adjacent exhaust line.\4\ The analysis, which addresses a potential 
    design deficiency in the HPCI barometric condenser, shows that the 
    containment penetration head fitting and interface piping will not 
    fail as a result of the water hammer associated with the HPCI start. 
    Since failure of the HPCI system is already considered in the plant 
    design-basis accident analysis; this is not a different type of 
    malfunction than that already considered.
    
    HPCI Relay Panel 1C620(2C620) & 250 V DC Control Center 1D264(2D264)
    
        No new failure modes are introduced by the hardware changes in 
    the 250 VDC Control Center 1D264 (2D264) and HPCI Relay Panel 1C620 
    (2C620). Some failure modes are eliminated by the proposed change. 
    Specifically, the potential failure of the HPCI suction auto-
    transfer on high suppression pool level is eliminated since that 
    logic is removed. Potential spurious auto-transfer associated with 
    high suppression pool logic is also eliminated. HPCI suction auto-
    transfer on low CST level and its potential to fail are unchanged by 
    this change.
        On a component level, potential failure modes for the AX relay 
    in 250 VDC Control Center 1D264 (2D264) are eliminated by this 
    modification because the relay is disconnected and removed by this 
    change. The potential failure modes for the relay K19 in panel 1C620 
    (2C620) are unchanged. Since the control functions of K19 have been 
    eliminated, the failure of the relay has no effect on HPCI suction 
    valve F042 operation.
        Removal of the relay from 250 VDC Control Center 1D264 (2D264) 
    and the replacement of the relay in the HPCI Relay Panel 1C620 
    (2C620) changes the load on the battery systems by a small amount. 
    The change in battery load and change in line voltage drop are 
    negligible and they do not adversely affect the performance of the 
    panels or battery systems. In addition, seismic qualification of the 
    panels is not adversely affected by this change.
    
    RCIC Turbine
    
        As discussed in the safety assessment for this change, the 
    proposed change has no adverse effects on RCIC turbine operation. 
    Therefore, the proposed change cannot result in a new RCIC failure 
    mode.
    
    Safety-Related Valves on Piping Connected to Suppression Chamber
    
        MOVs--The increased suppression pool water level which can occur 
    as a result of the proposed change does not create a failure 
    mechanism for safety-related valves on piping connected to the 
    suppression pool. The pressure differential for any valve on piping 
    connected to the suppression pool will increase by at most 0.86 psi. 
    This change in differential pressure has negligible effect on valve 
    operation.
        Vacuum Breakers--The proposed change cannot lead to malfunction 
    of the downcomer-vent vacuum breakers as the maximum level expected 
    in a design-basis event is 26 feet, and the vacuum breakers are 
    located at 42 feet above the suppression pool floor.
        SRVs/Tailpipes--There is no interaction between increased 
    suppression pool level and SRV operation since the flow through the 
    SRVs is choked and therefore decoupled from downstream conditions. 
    Also, the increased suppression pool level cannot lead to failure of 
    the SRV tailpipe because the potential level increase is well below 
    the SRV Tailpipe Level Limit.\5\ If suppression pool water level is 
    below this limit, there is no concern of tailpipe failure due to 
    overpressurization. The minimum value of the SRV Tailpipe Level 
    Limit is 35 feet.\6\ This is 9 feet above the maximum level expected 
    in a design-basis accident. For beyond-design-basis events, SRV 
    tailpipe integrity is protected by the EOP requirement to 
    depressurize the reactor on the SRV Tailpipe Level Limit.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Based on the following discussion for the containment, reactor 
    building, HPCI and RCIC system, and the safety-related valves in 
    piping connected to the suppression pool, the proposed action does 
    not involve a significant reduction in a margin of safety.
    
    HPCI System
    
        The HPCI Technical Specifications ensure that the system is 
    capable of providing adequate core cooling to limit clad 
    temperatures in the event of a small break LOCA which does not 
    result in rapid depressurization of the RPV (Technical Specification 
    Section 3/4.5.1 & 3/4.5.2). The proposed change has no adverse 
    affects on the injection capability of the HPCI system. Therefore, 
    the safety function of the system is not degraded, and there is no 
    reduction in the margin of safety as defined in the basis for the 
    HPCI Technical Specifications.
        Primary Containment and Reactor Building Safety-Related Systems, 
    Structures, and Components Affected by LOCA/SRV Hydrodynamic Loads
        Removal of the HPCI auto suction transfer on high suppression 
    pool level does not affect the Technical Specification requirement 
    to maintain suppression pool water level between 22 and 24 feet 
    (Technical Specification 3.6.2.1). Therefore, the maximum 
    containment pressure during the design-basis accident is unaffected 
    by the proposed change, and there can be no reduction in the margin 
    of safety as defined in the basis for Technical Specification
    
    [[Page 66716]]
    
    3.6.2.1. Furthermore, a detailed examination of the reactor and 
    containment response under accident and transient conditions 
    involving HPCI operation found no situations where the auto suction 
    transfer was necessary to maintain LOCA and SRV loads within the 
    design basis envelope. Therefore, from the standpoint of LOCA/SRV 
    hydrodynamic loads, the proposed change does not reduce the margin 
    of safety for any primary containment or reactor building structure, 
    system, or component.
    
    RCIC Turbine
    
        The basis for Technical Specification 3.7.3 states that the RCIC 
    system is provided to assure adequate core cooling in the event of a 
    reactor isolation with loss of feedwater flow. The proposed change 
    does not prohibit RCIC from performing this function, nor does it 
    degrade in any way the core cooling capability of RCIC. Therefore, 
    there is no reduction in the margin of safety as defined in the 
    basis for Technical Specification 3.7.3.
    
    Safety-Related Valves on Piping Connected to Suppression Pool
    
        MOVs--The increase in suppression pool water level which can 
    occur as a result of the proposed change does not reduce the margin 
    of safety for safety-related valves on piping connected to the 
    suppression pool. The pressure differential for any valve on piping 
    connected to the suppression pool will increase by at most 0.86 psi. 
    This change in differential pressure has negligible effect on valve 
    operation.
        Vacuum Breakers--The proposed change cannot reduce the margin of 
    safety as discussed in the basis for Technical Specification 3.6.4 
    because the maximum level expected in a design-basis event is 26 
    feet which is well below the downcomer-vent vacuum breaker elevation 
    of 42 feet.
        SRVs/Tailpipes--There is no interaction between increased 
    suppression pool level and SRV operation since the flow through the 
    SRVs is choked and therefore decoupled from downstream conditions. 
    Consequently, there is no reduction in the margin of safety as 
    defined in the bases for Technical Specifications 3.4.2 (safety 
    valve function) and 3.5.1.d (ADS function). Also, the increased 
    suppression pool level does not lead to a reduction in the margin of 
    safety for the SRV tailpipes because the tailpipes can operate 
    safely with pool levels up to 35 feet. This is nine feet above the 
    maximum suppression pool level that can occur in a design-basis 
    accident with the proposed change. For beyond-design-basis events, 
    SRV tailpipe integrity is protected by the EOP requirement to 
    depressurize the reactor on the SRV Tailpipe Level Limit.\7\
    
    HPCI Relay Panel 1C620(2C620) & 250 V DC Control Center 1D264(2D264)
    
        As discussed previously, removal of the relay from 250 VDC 
    Control Center 1D264 (2D264) and the replacement of the relay in the 
    HPCI Relay Panel 1C620 (2C620) changes the load on the battery 
    systems by a small amount. The change in battery load and change in 
    line voltage drop are negligible and therefore they do not reduce 
    the margin of safety for the panels or battery systems. In addition, 
    seismic qualification of the panels is not adversely affected by 
    this change so there is no reduction in the margin of safety for 
    seismic events.
        1. DBD041, Rev. 0, p. 1. [design basis document for RCIC system]
        2. SSES DAR [design assessment report for suppression pool 
    hydrodynamic loads], Section 9.4.1
        3. Suppression pool level must be maintained less than 24 feet 
    in accordance with Technical Specification 3.6.2.1.a.
        4. GKR-03-001, ``NRC and Utility Notification of Closeout of GE 
    PRC92-05, Potential Design Deficiency on HPCI,'' January 6, 1993 [GE 
    letter to PP&L regarding closure of HPCI design issue].
        5. This limit is defined in EO-100/200-103 [emergency operating 
    procedure]
        6. Bechtel Calculations PUP-15598-S2 & PUP-15598-S6, and PLE-
    15315 (March 2, 1992)
        7. The limit is defined in EO-100/200-103 [emergency operating 
    procedure]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: October 7, 1996.
        Description of amendment request: The amendments would modify the 
    Susquehanna Steam Electric Station, Units 1 and 2, Technical 
    Specifications by revising the trip setpoints and allowable values for 
    the secondary containment isolation ``Refuel Floor High Exhaust Duct 
    Radiation--High'' monitor, the ``Railroad Access Shaft Exhaust Duct 
    Radiation--High'' monitor, and the ``Refuel Floor Wall Exhaust Duct 
    Radiation--High'' monitor in Table 3.3.2-2. The change would enhance 
    the operational efficiency of plant operations by eliminating 
    compensatory measures which prevent spurious secondary containment 
    isolations, and initiation of the standby gas treatment system (SGTS) 
    and recirculation system during refueling activities. This change would 
    also allow for the use of the hydrogen water chemistry system during 
    operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change to the trip setpoints and allowable values 
    to the ``Refuel Floor High Exhaust Duct Radiation--High'' monitor, 
    the ``Railroad Access Shaft Exhaust Duct Radiation--High'' monitor, 
    and the ``Refuel Floor Wall Exhaust Duct Radiation--High'' monitor 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The design basis 
    for the monitors is to monitor radiation in the unfiltered air from 
    the Zone III exhaust system to provide signals which isolate the 
    Zone III of the secondary containment on a high radiation condition, 
    and to initiate SGTS and the Recirculation system to limit offsite 
    doses to maintain regulatory requirements.
        The original setpoints for these monitors were based upon normal 
    radiological operating conditions and were set at a value to 
    preclude spurious design actuations by these monitors during normal 
    plant operations. However, the monitors are designed to detect 
    radiation associated with certain postulated accident conditions. As 
    required by the Technical specifications the monitors are operable 
    when conditions exist that may result in fuel damage events, and 
    therefore, will perform their design basis function. Consequently, 
    an increase to the trip setpoints and allowable values is warranted 
    since the existing setpoints, which are conservatively based on 
    normal radiological operating conditions, are not related to the 
    design basis of the monitors. Therefore, based upon the design basis 
    of the monitors, an increase to the trip setpoints and allowable 
    values will not result in a decrease of the safety function of the 
    monitors but will make the trip setpoints and allowable values 
    consistent with the design basis.
        Based on the design basis of these monitors, revised analytical 
    limits were derived reflecting the accident function of the 
    monitors. The analytical limit calculations utilized FSAR realistic 
    source terms, instead of the worst case source terms utilized for 
    10CFR [Part] 100 compliance. Use of the realistic source terms 
    results in conservative analytical limits.
        The ``Refuel Floor High Exhaust Duct Radiation--High'' monitor, 
    and the ``Refuel Floor Wall Exhaust Duct Radiation--High'' [monitor] 
    are required to be OPERABLE during CORE ALTERATIONS (except for 
    single control rod movements unless performing TS 3.10.3), 
    operations with the potential for draining the reactor vessel, and 
    handling of irradiated fuel in the secondary containment. The 
    ``Railroad Access Shaft Exhaust Duct Radiation--High'' monitor is 
    required to be operable during handling of irradiated fuel. These 
    Technical Specification
    
    [[Page 66717]]
    
    applicable operational conditions for the monitors are not affected 
    since this proposed revision only revises the trip setpoints and 
    allowable values to be consistent with the design bases of the 
    monitors.
        For the reasons stated above the revisions to the trip setpoints 
    and allowable values to the ``Refuel Floor High Exhaust Duct 
    Radiation--High'' monitor, the ``Railroad Access Shaft Exhaust Duct 
    Radiation--High'' monitor, and the ``Refuel Floor Wall Exhaust Duct 
    Radiation--High'' monitor in Technical Specification.
        Table 3.3.2-2 can be implemented without a significant increase 
    in the probability or consequence of an accident previously 
    evaluated.
        II. This proposal does not create the possibility of a new or 
    different kind of accident previously evaluated.
        The proposed change to the trip setpoints and allowable values 
    for the ``Refuel Floor High Exhaust Duct Radiation--High'' monitor, 
    the ``Railroad Access Shaft Exhaust Duct Radiation--High'' monitor, 
    and the ``Refuel Floor Wall Exhaust Duct Radiation--High'' monitor 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The monitors are designed to limit the release of airborne 
    radioactivity in the secondary containment Zone III exhaust system 
    by isolating Zone III, initiating [the] SGTS and initiating the 
    Recirculation System on high radiation resulting from fuel handling 
    accidents. Therefore, the design basis for these monitors is to 
    monitor radiation in the unfiltered air from the Zone III exhaust 
    system, and provide signals to limit offsite doses to maintain 
    regulatory requirements. Zone III includes the Refueling Floor and 
    can include the Railroad Access Shaft during certain alignments. 
    These radiation monitors are not provided for occupational 
    protection associated with operational radiation doses. The proposed 
    revision does not affect the design basis of the monitors nor the 
    kind of accident associated with the basis; therefore, no potential 
    to create a new or different accident exists.
        For the reasons stated above the revisions to the trip setpoints 
    and allowable values to the ``Refuel Floor High Exhaust Duct 
    Radiation--High'' monitor, the ``Railroad Access Shaft Exhaust Duct 
    Radiation--High'' monitor, and the ``Refuel Floor Wall Exhaust Duct 
    Radiation--High'' monitor in Technical Specification Table 3.3.2-2 
    can be implemented without creating the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        III. This proposal does not involve a significant reduction on a 
    margin of safety.
        The proposed change to the trip setpoints and allowable values 
    for the ``Refuel Floor High Exhaust Duct Radiation--High'' monitor, 
    the ``Railroad Access Shaft Exhaust Duct Radiation--High'' monitor, 
    and the ``Refuel Floor Wall Exhaust Duct Radiation--High'' monitor 
    does not involve a significant reduction in a margin of safety.
        The monitors are designed to limit the release of airborne 
    radioactivity in the secondary containment Zone III exhaust system 
    by isolating Zone III, initiating [the] SGTS and initiating the 
    Recirculation System on high radiation resulting from fuel handling 
    accidents. Therefore, the design basis for these monitors is to 
    monitor radiation in the unfiltered air from the Zone III exhaust 
    system, and provide signals to limit offsite doses to maintain 
    regulatory requirements. Zone III includes the Refueling Floor and 
    can include the Railroad Access Shaft during certain alignments. 
    These radiation monitors are not provided for occupational 
    protection associated with operational radiation doses. However, the 
    original setpoints for these monitors were conservatively based upon 
    normal radiological operating conditions and were set at a value to 
    preclude spurious design actuation by these monitors during normal 
    plant operations. The calculations performed to support the trip 
    setpoint and allowable value revisions concluded that the change 
    will maintain offsite doses within the 10CFR100 limits. The ``Refuel 
    Floor High Exhaust Duct Radiation--High'' monitor, and the ``Refuel 
    Floor Wall Exhaust Duct Radiation--High'' are required to be 
    OPERABLE during CORE ALTERATIONS (except for single control rod 
    movements unless performing TS 3.10.3), operations with the 
    potential for draining the reactor vessel, and handling of 
    irradiated fuel in the secondary containment. The ``Railroad Access 
    Shaft Exhaust Duct Radiation--High'' monitor is required to be 
    operable during handling of irradiated fuel. These Technical 
    Specification applicable operational conditions for the monitors are 
    not affected since the proposed revision only revises the trip 
    setpoints and allowable values to be consistent with the design 
    bases of the monitors.
        The proposed revisions to the trip setpoints and allowable 
    values, in addition to being based on the appropriate accident 
    conditions, were also developed utilizing standard setpoint change 
    methodologies that consider instrument and calibration accuracies 
    and instrument drift tolerances. This provides added conservatism to 
    assure that the revised trip setpoints and allowable values are not 
    exceeded.
        For the reasons stated above the revisions to the trip setpoints 
    and allowable values to the ``Refuel Floor High Exhaust Duct 
    Radiation--High'' monitor, the ``Railroad Access Shaft Exhaust Duct 
    Radiation--High'' monitor, and the ``Refuel Floor Wall Exhaust Duct 
    Radiation--High'' monitor in Technical Specification Table 3.3.2-2 
    can be implemented without involving a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania.
    
        Date of amendment request: November 25, 1996.
        Description of amendment request: The proposed Technical 
    Specifications (TS) changes would revise the wording in TS Section 
    4.8.1.1.2.e.2 and the associated TS Bases Section 3/4.8 to remove the 
    specific reference to the Residual Heat Removal pump motor and its 
    corresponding kW rating value, and replace it with wording consistent 
    with that specified in the Improved TS (i.e., NUREG-1433, Revision 1, 
    ``Standard Technical Specifications General Electric Plants,'' dated 
    April 1995).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS changes do not make any physical alterations or 
    modifications to the plant systems or equipment. The proposed 
    changes do not adversely impact the operation of any plant 
    equipment. The EDGs will continue to function as designed to ensure 
    that the necessary electrical power is provided to essential plant 
    equipment to mitigate the consequences of an accident, e.g., Loss-
    of-Offsite-Power (LOOP) and Loss-of-Coolant Accident LOCA) 
    coincident with a LOOP (LOCA/LOOP). The proposed TS changes do not 
    impact the performance testing requirements associated with the 
    EDGs. The accident mitigating capabilities of the diesel generators 
    and emergency loads will remain the same.
        The proposed TS changes are consistent with the guidance 
    stipulated in NUREG-1433, Revision [1], ``Standard Technical 
    Specification General Electric Plants,'' regarding single load 
    rejection testing of the EDGs. Specifically, the proposed changes 
    involve revising the wording in TS Surveillance Requirement (SR) 
    4.8.1.1.2.e.2 to remove the specific reference to the Residual Heat 
    Removal (RHR) pump motor and associated kW loading value (992 kW), 
    and replace it with wording indicating that the EDGs must be capable 
    of rejecting the single largest post-accident load, which is 
    consistent with NUREG-1433, Revision 1, guidance. The proposed 
    changes will also provide additional flexibility for future plant 
    maintenance activities.
        Each EDG will continue to be tested by rejecting a load of 
    greater than or equal to that of its single largest post-accident 
    load while maintaining voltage and frequency
    
    [[Page 66718]]
    
    within the current specified parameters. The RHR pump motors are 
    currently used in performing the EDG single load rejection testing. 
    The RHR pump motors will continued [sic] [continue] to be used in 
    performing the surveillance testing since they are the single 
    largest post-accident electrical load. The consequences of a 
    malfunction of equipment are not affected. Failure of a EDG or its 
    safety-related loads is bounded by the loss of a Class 1E electrical 
    power division which has been previously evaluated as discussed in 
    LGS Updated Final Safety Analysis Report (UFSAR) Sections 8.1.5.2.e 
    and 8.3.1.1.3.
        Therefore, the proposed TS changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes do not make any physical alterations or 
    modifications to the plant systems or equipment. The proposed 
    changes do not adversely impact the operation of any plant 
    equipment. The EDGs will continue to function as designed to provide 
    essential electrical power to mitigate the consequences of an 
    accident. The proposed TS changes are consistent with the guidance 
    stipulated in NUREG-1433, Revision 1, regarding single load 
    rejection testing of the EDGs. The proposed changes do not introduce 
    any new accidents or transients. The proposed TS changes will 
    provide additional flexibility for future maintenance activities. 
    The proposed changes do not alter any EDG testing requirements or 
    frequencies. The RHR pump motors are currently used in performing 
    the EDG single load rejection testing. The RHR pump motors will 
    continue to be used in performing the surveillance testing since 
    they are the single largest post-accident electrical load. The 
    operation of the EDGs and their corresponding safety-related 
    electrical loads remain unchanged as a result of the proposed TS 
    changes.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The proposed TS changes do not involve any physical changes to 
    plant systems or equipment. The proposed TS changes are consistent 
    with the guidance stipulated in NUREG-1433, Revision 1, ``Standard 
    Technical Specification General Electric Plants,'' regarding single 
    load rejection testing of the EDGs. The proposed TS changes will 
    provide additional flexibility for future plant maintenance 
    activities. The EDGs will continue to function as designed to 
    provide essential electrical power to mitigate the consequences of 
    an accident. The operation of the EDGs and their corresponding 
    safety-related electrical loads remain unchanged as a result of the 
    proposed TS changes.
        Therefore, the proposed TS changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, PA 19101.
        NRC Project Director: John F. Stolz.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
    364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, 
    Alabama
    
        Date of amendments request: November 15, 1996.
        Description of amendments request: The amendments would eliminate 
    the containment systems Technical Specification 3.6.2.2. ``Spray 
    Additive System.'' The specification would be replaced with a new 
    emergency core cooling system Technical Specification 3.5.6 ``ECCS 
    Recirculation Fluid pH Control System.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The proposed change involves replacement of concentrated 
    NaOH injected via the containment spray system with trisodium 
    phosphate (TSP) stored in the containment and dissolved in the sump 
    recirculation solution to maintain acceptable post accident spray/
    recirculation solution chemistry. Deletion of the concentrated NaOH 
    will eliminate a personnel hazard. The pH control system functions 
    in response to an accident and does not involve or have any effect 
    on any initiating event for any accident previously evaluated. 
    Operation under the proposed amendments will continue to ensure that 
    iodine potentially released post-LOCA [loss-of-coolant accident] is 
    retained in the sump solution, and resultant offsite and control 
    room thyroid doses are within the limits of 10 CFR [Part] 100 and 10 
    CFR [Part] 50, Appendix A, General Design Criterion [GDC] 19, 
    respectively.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The deleted equipment is isolated from the remaining 
    equipment by cut-and-capped piping, determinated and/or spared 
    cables; and interfaces are analyzed to ensure the remaining required 
    equipment meets applicable original design requirements. The new 
    equipment (TSP and baskets) is a passive pH control system and is 
    supported and analyzed to ensure there are no adverse interfaces 
    (e.g., pipe break, jet impingement, seismic) with existing 
    equipment, system, or structures.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety. The slight change in recirculation solution 
    pH maintains adequate protection against chloride and caustic 
    induced stress corrosion cracking on mechanical systems and 
    components, and maintains the capability of the solution to retain 
    iodine. It does not result in a change to the hydrogen generation 
    analysis for containment. The increased mass inside containment will 
    have no significant impact on post-accident flood levels, 
    recirculation solution boron concentration, or peak clad 
    temperatures. No other operating parameters for systems, structures, 
    or components assumed to operate in the safety analysis are changed. 
    The offsite and control room doses meet the limits of 10 CFR [Part] 
    100 and GDC 19, respectively. Because the trisodium phosphate is 
    nonvolatile and the baskets are protected with solid covers and are 
    located slightly above the floor in the containment where access is 
    strictly controlled, a surveillance interval of once per refueling 
    outage provides assurance that the TSP will be available.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201.
        NRC Project Director: Herbert N. Berkow.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued
    
    [[Page 66719]]
    
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: June 3, 1996, as supplemented October 
    23, 1996.
        Description of amendment request: The proposed amendment would 
    clarify a restriction on shutdown margin monitor operability while 
    changing modes so that it only limits reactivity changes caused by 
    boron dilution and rod withdrawal.
        Date of publication of individual notice in Federal Register: June 
    20, 1996 (61 FR 31559).
        Expiration date of individual notice: July 22, 1996.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station Units 1 and 2, Lake County, Illinois
    
        Date of application for amendments: October 4, 1996 and 
    supplemented on November 6, 1996.
        Brief description of amendments: The amendments add a Mode of 
    Applicability to Technical Specification 3.2.3.D, Inoperable Rod 
    Position Indicator Channels.
        Date of issuance: November 25, 1996.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 176 and 163.
        Facility Operating License Nos. DPR-39 and DPR-48: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 17, 1996 (61 FR 
    54240).
        The November 6, 1996, submittal provided additional clarifying 
    information that did not affect the Commission's initial proposed 
    finding of no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 25, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: June 21, 1996.
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) Section 3/4.9.6, ``Manipulator Crane,'' to make the 
    wording consistent with the TS Bases description and consistent with 
    the design of the load handling equipment.
        Date of issuance: November 25, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 156 and 148.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55031) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 25, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: September 17, 1996 (TSC 96-01) 
    as supplemented October 23, 1996.
        Brief description of amendments: The amendments lower the maximum 
    allowable reactor building pressure, lower the actuation setpoint for 
    actuation of the reactor building spray system, and modify the 
    associated TS Bases requirements.
        Date of Issuance: November 25, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 219, 219, 216.
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55031). The October 23, 1996, letter provided clarifying information 
    that did not change the scope of the September 17, 1996, application 
    and the initial proposed no signficant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 25, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691.
    
    [[Page 66720]]
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Entergy Mississippi, Inc., 
    Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, Claiborne 
    County, Mississippi
    
        Date of application for amendment: July 31, 1996, as supplemented 
    by letters of September 5, October 22, and November 15, 20, and 21, 
    1996, which supersede the application submitted in the letter of May 9, 
    1996.
        Brief description of amendment: The amendment (1) increased the 
    safety limit minimum critical power ratio (MCPR) for two loop operation 
    and single loop operation to 1.12 and 1.14, respectively, and (2) added 
    two General Electric topical reports to the list of documents 
    describing the analytical methods used to determine the core operating 
    limits. The changes are to Section 2.1.1, Reactor Core Safety Limits, 
    and Section 5.6.5, Core Operating Limits Report (COLR), respectively, 
    of the Technical Specifications. This amendment would go into effect in 
    Operating Cycle 9, at the end of the current Refueling Outage 8, and 
    the plant will have a mixed core of Siemens Power Corporation (SPS) 
    9 x 9-5 and General Electric (GE) GE11 reload fuel. The licensee also 
    changed the Bases of the Technical Specifications associated with the 
    above amendment.
        Date of issuance: November 21, 1996.
        Effective date: November 21, 1996.
        Amendment No: 131.
        Facility Operating License No. NPF-29: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 25, 1996.The 
    October 22, and November 15, 20, and 21, 1996, submittals provide 
    clarifying information that did not change the initial determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated November 21, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: April 15, 1996 (TSCR No. 244).
        Brief description of amendment: The amendment revises Specification 
    5.3.1.B to allow the shield plug and the associated lifting hardware to 
    be moved over irradiated fuel assemblies that are in a dry shielded 
    canister within the transfer cask in the cask drop protection system.
        Date of Issuance: November 7, 1996.
        Effective date: November 7, 1996, to be implemented within 30 days 
    of issuance.
        Amendment No.: 187.
        Facility Operating License No. DPR-16: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 8, 1996 (61 FR 
    20849). The Commission's related evaluation of this amendment and final 
    determination of no significant hazards consideration addressing 
    comments received on the proposed no significant hazards consideration 
    determination are contained in a Safety Evaluation dated November 7, 
    1996.
        No significant hazards consideration comments received: Yes.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket No. 
    50-461, Clinton Power Station, Unit No. 1, DeWitt County, Illinois
    
        Date of application for amendment: February 22, 1996, and as 
    supplemented by letters dated July 24, October 4, November 19 and 
    November 25, 1996.
        Brief description of amendment: The amendment changes Clinton Power 
    Station Technical Specification (TS) 3.3.8.1, ``Loss of Power 
    Instrumentation,'' and TS 3.8.1, ``AC Sources-Operating,'' by revising 
    the setpoint for the degraded voltage protection instrumentation and 
    modifying or deleting other Loss of Power Instrumentation TS 
    requirements. In addition, changes were also made to the minimum 
    required diesel generator voltage specified for certain diesel 
    generator surveillances.
        Date of issuance: December 4, 1996.
        Effective date: December 4, 1996.
        Amendment No.: 110.
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18168).The letters of July 24, October 4, November 19 and November 25, 
    1996, provided clarifying information and did not represent significant 
    changes from the original Federal Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated December 4, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of application for amendments: October 11, 1996.
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) 3.9.6, ``Refueling Water Level,'' for San Onofre 
    Nuclear Generating Station (SONGS), Units 2 and 3. The proposed change 
    is required to restore certain provisions of the SONGS Units 2 and 3 
    operating practice that were not incorporated during the conversion to 
    the improved TS (Amendment Nos. 127 and 116, dated February 9, 1996).
        Date of issuance: December 3, 1996.
        Effective date: December 3, 1996, to be implemented within 30 days 
    from the date of issuance.
        Amendment Nos.: Unit 2--134; Unit 3--123.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 31, 1996 (61 FR 
    56251) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated December 3, 1996.
        No significant hazards consideration comments received: No.
        Temporary Local Public Document Room location: Science Library, 
    University of California, P.O. Box 19557, Irvine, California 92713.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 24, 1995, as supplemented by 
    letter dated July 26, 1996.
        Brief description of amendment: The amendment revised Technical 
    Specification (TS) Surveillance Requirement 4.5.1.1.a.1 to base 
    accumulator operability on actual parameters (i.e., borated water 
    volume and nitrogen cover-pressure in the tanks) vs. the absence of 
    alarms.
        Date of issuance: November 22, 1996.
        Effective date: November 22, 1996, to be implemented within 30 days 
    of issuance.
        Amendment No.: 103.
        Facility Operating License No. NPF-42: The amendment revised the 
    Technical Specifications.
    
    [[Page 66721]]
    
        Date of initial notice in Federal Register: April 12, 1995 (60 FR 
    18632) The July 26, 1996, letter provided additional clarifying 
    information and did not change the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated November 22, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
        Dated at Rockville, Maryland, this 11th day of December 1996.
    
        For the Nuclear Regulatory Commission.
    Steven A. Varga,
    Director, Division of Reactor Projects--I/II, Office of Nuclear Reactor 
    Regulation.
    [FR Doc. 96-31944 Filed 12-17-96; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
12/18/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-31944
Dates:
Immediately, to be implemented within 30 days.
Pages:
66702-66721 (20 pages)
PDF File:
96-31944.pdf