94-31308. Philadelphia Electric Company; Limerick Generating Station, Units 1 and 2 Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 59, Number 244 (Wednesday, December 21, 1994)]
    [Unknown Section]
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    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 94-31308]
    
    
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    [Federal Register: December 21, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-352 and 50-353]
    
     
    
    Philadelphia Electric Company; Limerick Generating Station, Units 
    1 and 2 Environmental Assessment and Finding of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of an exemption to Facility Operating License Nos. 
    NPF-39 and NPF-85, issued to Philadelphia Electric Company (the 
    licensee), for operation of the Limerick Generating Station (LGS), 
    Units 1 and 2, located in Montgomery County, Pennsylvania.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed action would grant an exemption from 10 CFR Part 50, 
    Appendix J, ``Primary Reactor Containment Leakage Testing for Water-
    Cooled Power Reactors,'' Sections III.D.2(a) and III.D.3, which require 
    that Type B and C containment penetration leak rate tests be performed 
    during reactor shutdown for refueling, or other convenient intervals, 
    but in no case greater than 2 years. The licensee requests that, this 
    one-time exemption would allow the two-year interval to be exceeded by 
    no more than 26 days and not to surpass February 19, 1995.
        The proposed action is in accordance with the licensee's 
    application for exemption dated July 22, 1994.
    
    The Need for the Proposed Action
    
        The affected containment penetrations must be leak rate tested 
    (either Type B or C test) during shutdown reactor conditions because 
    testing of the penetrations requires access to the drywell or requires 
    isolation of safety systems. The required leak rate test intervals for 
    the affected penetrations listed on the licensee's exemption request 
    will exceed the 2-year maximum test interval, if not tested between 
    January 24, 1995 and February 18, 1995.
        The licensee's upcoming refueling outage is scheduled to begin on 
    January 28, 1995. The licensee has proposed the exemption to extend the 
    leak test interval for the affected penetrations by no more than 26 
    days. This will allow the licensee to avoid shutting down 4 days 
    earlier for the sole purpose of conducting Appendix J Type B and C 
    tests. The proposed action will permit the licensee to have flexibility 
    to schedule the leak rate tests within the upcoming outage time period.
    
    Environmental Impacts of the Proposed Action
    
        The licensee has presented information in support of their request 
    for a 26-day extension of the Type B and C test intervals. The Unit 2, 
    as-left minimum pathway leak rate (i.e., maximum allowable leakage rate 
    for maintaining primary containment), following the second Unit 2 
    refueling outage, was .13 La (maximum allowable pathway leakage) 
    or 20,625 standard cubic centimeters per minute (sccm), including 
    contributions from the Main Steam Isolation Valves (MSIV); with a 
    maximum pathway leak rate of .27 La or 42,502 sccm, excluding MSIV 
    leakage, in accordance with LGS's current Appendix J exemption. These 
    as-left leak rates represent a significant margin to the maximum 
    allowable pathway leakage of 158,273 sccm.
        The Commission has completed the evaluation to the proposed action 
    and concludes that this action would not significantly increase the 
    probability of exceeding the maximum allowable value of expected 
    primary containment leakage during a hypothetical design basis 
    accident. Performing the Type B and C tests for the specified 
    penetrations no more than 26 days beyond the 2-year interval, not to 
    exceed February 19, 1995, would meet the underlying purpose of the 
    rule, that any primary containment leakage during a hypothetical design 
    basis accident will remain less than the maximum allowable leakage rate 
    value established by 10 CFR Part 50, Appendix J.
        Thus, radiological releases will not differ from those determined 
    previously and the proposed action does not otherwise affect facility 
    radiological effluent or occupational exposures. The change will not 
    increase the probability or consequences of accidents, since no changes 
    are being made in the types of any effluents that may be released 
    offsite, and there is no significant increase in the allowable 
    individual or cumulative occupational radiation exposure. Accordingly, 
    the Commission concludes that there are no significant radiological 
    environmental impacts associated with the proposed action.
        With regard to potential nonradiological impacts, the proposed 
    action involves a one-time schedular change to surveillance and testing 
    requirements that does not affect nonradiological plant effluents and 
    has no other environmental impact. Accordingly, the Commission 
    concludes that there are no significant nonradiological environmental 
    impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there is no measurable 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated. The principal alternative to the action would be to deny the 
    request. Such action would not enhance the protection of the 
    environment and would result in no change in current environmental 
    impacts. The environmental impact of the proposed action and the 
    alternative action are similar.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the ``Final Environmental Statement related to 
    the operation of Limerick Generating Station, Units 1 and 2,'' dated 
    April 1984.
    
    Agencies and Persons Consulted
    
        The NRC staff consulted with the Pennsylvania State official 
    regarding the environmental impact of the proposed action. The State 
    official had no comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated July 22, 1994, which is available for public 
    inspection at the Commission's Public Document Room, The Gelman 
    Building, 2120 L Street, NW., Washington, DC, and the local public 
    document room located at the Pottstown Public Library, 500 High Street, 
    Pottstown, Pennsylvania 19464.
    
        Dated at Rockville, Maryland, this 15th day of December 1994.
        For the Nuclear Regulatory Commission.
    Chester Poslusny,
    Acting Director, Project Directorate I-2, Division of Reactor 
    Projects--I/II, Office of Nuclear Reactor Regulation.
    [FR Doc. 94-31308 Filed 12-20-94; 8:45 am]
    BILLING CODE 7590-01-M
    
    
    

Document Information

Published:
12/21/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-31308
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: December 21, 1994, Docket Nos. 50-352 and 50-353