98-34440. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 63, Number 250 (Wednesday, December 30, 1998)]
    [Notices]
    [Pages 71962-71984]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-34440]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from December 7, 1998, through December 17, 1998. 
    The last biweekly notice was published on December 16, 1998 (63 FR 
    69332).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or
    
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    different kind of accident from any accident previously evaluated; or 
    (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By January 29, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    [[Page 71964]]
    
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of amendment request: October 27, 1998.
        Description of amendment request: The Carolina Power & Light 
    Company, licensee for the Brunswick Steam Electric Plant (BSEP), Unit 
    Nos. 1 and 2, proposed amendments to the Operating Licenses for the 
    BSEP units. The amendments are administrative in nature and would 
    delete various completed license conditions, make editorial changes, 
    and provide clarifying information.
        The licensee has concluded that the proposed license amendments do 
    not involve a Significant Hazards Consideration. In support of this 
    determination, an evaluation of each of the three standards set forth 
    in 10 CFR 50.92 is provided below.
        Basis for a proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed license amendments do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes revise the BSEP, Unit Nos. 1 and 2, Facility 
    Operating Licenses to delete various license conditions that have been 
    completed, make editorial changes, and provide clarifying information. 
    The changes are administrative and only provide updated and clarifying 
    information. No physical or operational changes to the facility will 
    result from the proposed changes. Therefore, the proposed license 
    amendments do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed license amendments will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes revise the BSEP, Unit Nos. 1 and 2, Facility 
    Operating Licenses to delete various license conditions that have been 
    completed, make editorial changes, and provide clarifying information. 
    The changes are administrative and only provide updated and clarifying 
    information. The proposed license amendments do not alter any plant 
    operation and will not result in a physical change to the facility. 
    Therefore, the proposed license amendments do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed license amendments do not involve a significant 
    reduction in a margin of safety.
        The proposed changes revise the BSEP, Unit Nos. 1 and 2, Facility 
    Operating Licenses to delete various license conditions that have been 
    completed, make editorial changes, and provide clarifying information. 
    The changes are administrative and only provide updated and clarifying 
    information. No physical or operational changes to the facility will 
    result from the proposed changes. Therefore, the proposed license 
    amendments do not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Frederick J. Hebdon.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois, Docket 
    Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 1 and 
    2, Rock Island County, Illinois
    
        Date of application for amendment request: November 30, 1998.
        Description of amendment request: This amendment request proposes 
    to relocate, to a licensee controlled document, the requirement for 
    removal of the Reactor Protection System (RPS) shorting links. Removal 
    of the shorting links enables a non-coincident scram on high neutron 
    flux as detected by the Source Range Monitors (SRMs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Does the change involve a significant increase in the probability 
    or consequences of an accident previously evaluated?
        The RPS shorting links are not precursors to any previously 
    evaluated accident. The Source Range Monitors (SRMs), and the ability 
    of the SRMs to provide a RPS trip, are also not precursors to any 
    previously evaluated accident. Therefore, relocating the RPS shorting 
    link requirement to administrative controls [the Updated Final Safety 
    Analysis Report (UFSAR)] will not increase the probability of an 
    accident previously evaluated.
        The RPS shorting links are not assumed to be removed in any 
    accident analysis, and the SRMs are not assumed to provide a RPS trip 
    in any accident analysis. The refueling interlocks and SHUTDOWN MARGIN 
    calculations will continue to provide assurance of reactivity control. 
    Therefore, relocating the RPS shorting link requirements to 
    administrative controls [the UFSAR] will not increase the consequences 
    of an accident previously evaluated.
        The RPS shorting link requirements will be relocated to 
    administrative controls that are administered pursuant to the 
    requirements of 10 CFR 50.59, thereby reducing the level of regulatory 
    control. The level of regulatory control has no impact on the 
    probability or consequences of an accident previously evaluated.
        Consequently, this proposed amendment does not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        Does the change create the possibility of a new or different kind 
    of accident from any accident previously evaluated?
        Relocating the RPS shorting link requirements to administrative 
    controls [the UFSAR] does not create any new failure mechanisms. No new 
    equipment will be installed or utilized, and no new operating 
    conditions will be initiated as a result of this change. Therefore, the 
    proposed change does not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        Does the change involve a significant reduction in a margin of 
    safety?
        The refuel interlocks and SHUTDOWN MARGIN calculations will 
    continue to ensure that the reactor stays
    
    [[Page 71965]]
    
    subcritical in the Refuel Mode. The margin to safety as represented by 
    the SHUTDOWN MARGIN designed into the core and verified in the SHUTDOWN 
    MARGIN calculations will be unaffected by relocation of the RPS 
    shorting link requirements to administrative controls [the UFSAR]. The 
    margin to safety as represented by the fuel bundle drop assumptions 
    protected by the refuel interlocks will be unaffected. In addition, no 
    accident analysis assumes that the RPS shorting links are removed. In 
    addition, the RPS shorting link requirements will be relocated to 
    administrative controls [the UFSAR] for which future change will be 
    evaluated pursuant to the requirements of 10 CFR 50.59. Therefore, 
    there will be no change in the types or significant increase in the 
    amounts of any effluents released offsite, and, thus, these changes do 
    not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments requested involve no significant hazards consideration.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Stuart A. Richards.
    
    Florida Power Corporation, et al. (FPC), Docket No. 50-302, Crystal 
    River Nuclear Generating Plant, Unit No. 3 (CR-3), Citrus County, 
    Florida
    
        Date of amendment request: October 30, 1998 (LAR-236).
        Description of amendment request: The proposed amendment would 
    change the Crystal River Unit 3 (CR-3) Improved Technical 
    Specifications (ITS) Section 5.6.2.19, Section 3.4.11, Bases 3.4.11 and 
    Bases 3.4.3. The changes reflect the use of fluence methodology 
    described in Topical Report BAW-2241P, ``Fluence and Uncertainty 
    Methodologies,'' and the use of American Society of Mechanical 
    Engineers (ASME) Code Case N-514, ``Low Temperature Overpressure 
    Protection,'' for developing Low Temperature Overpressure Protection 
    (LTOP) limits. Reference to Topical Report BAW-1543A, ``Integrated 
    Reactor Vessel Surveillance Program,'' was also added to ITS Section 
    5.6.2.19. ITS Section 3.4.11 (Low Temperature Overpressure Protection 
    System), was revised to reflect the new LTOP limits based on revised 
    fluence projections through 32 Effective Full Power Years (EFPY). The 
    Pressure/Temperature (P/T) Limits Report is being revised to reflect 
    the new P/T limits for heatup, cooldown, hydrostatic and leak test, and 
    to incorporate the CR-3 LTOP curve.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        LAR [License Amendment Request] #236 proposes several changes to 
    the ITS operational limits. These changes are being proposed to 
    maintain the necessary margins of safety through 32 EFPY using analyses 
    based on methodologies that have been previously approved for use at 
    CR-3, ASME Code Case N-514 and LTOP SER [Safety Evaluation Report], and 
    are currently being reviewed by the NRC staff:
    
    --NRC to FPC letter, 3N1293-30, dated December 20, 1993, ``Crystal 
    River Unit 3--Issuance of Amendment RE: Improved Technical 
    Specifications (TAC No. M74563)''
    --NRC to FPC letter, 3N1297-16, dated December 22, 1997, ``Crystal 
    River Unit 3--Staff Evaluation and Issuance of Amendment RE: Low-
    Temperature Overpressure Protection (TAC No. M99277)''
    --NRC to FPC letter, 3N079705, dated July 3, 1997, ``Crystal River 3--
    Exemption from Requirements of 10 CFR 50.60, Acceptance Criteria for 
    Fracture Prevention for Lightwater Nuclear Power Reactors for Normal 
    Operation (TAC No. M98380)''
    --BAW-2241P, ``Fluence and Uncertainty Methodologies''
    
        The limiting transient for LTOP remains a failed-open makeup valve. 
    Existing LTOP controls (maximum of one makeup pump capable of injecting 
    into the RCS [reactor coolant system], high pressure injection (HPI) 
    deactivated, the CFTs [core flood tanks] isolated, pressure relief 
    capability and maintaining a gas volume in the RCS) remain unchanged 
    from the current ITS 3.4.11 as approved by Reference 3, except the 
    setpoints proposed herein. The setpoints are being updated to reflect 
    the new 32 EFPY fluence analysis and P/T limits. Therefore, this change 
    does not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes will not create the possibility of a new or 
    different kind of accident from any previously evaluated since they do 
    not introduce new systems, failure modes or plant perturbations. 
    Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes will not involve a significant reduction in 
    the margin of safety since the proposed P/T limitations have been 
    developed consistent with the requirements of 10 CFR 50.60. The 
    operational limits have been developed to maintain the necessary 
    margins of safety as defined by ASME through 32 EFPY using 
    methodologies previously reviewed and approved by the NRC. The 
    objective of these limits is to prevent non-ductile failure during any 
    normal operating condition, including anticipated operational 
    occurrences and system hydrostatic tests.
        The LTOP safety factors are based on reanalyzed conditions for 32 
    EFPY of operation utilizing methodology contained in ASME Code Case N-
    514 which has been approved for use at CR-3. The Code Case provides an 
    acceptable margin of safety against flaw initiation and reactor vessel 
    failure. The application of Code Case N-514 for CR-3 ensures an 
    acceptable level of safety. Therefore, this change does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
        Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC-A5A, P. O. Box 14024, St. Petersburg, Florida 
    33733-4042.
        NRC Project Director: Frederick J. Hebdon.
    
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    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3 (CR-3), Citrus County, Florida
    
        Date of amendment request: October 30, 1998.
        Description of amendment request: The proposed amendment requests 
    approval of a change to the Crystal River Unit 3 (CR-3) Final Safety 
    Analysis Report (FSAR) regarding the methodology for performing the 
    Spent Fuel Pool (SFP) B criticality analysis. Recent Boraflex samples 
    from the SFP B demonstrate a weight loss in excess of the available 
    margin within the current licensing basis calculation. The criticality 
    analysis calculations proposed in this amendment request demonstrate 
    that the burnup/enrichment curves in the current Improved Technical 
    Specifications (ITS) have sufficient margin to accommodate up to a 20% 
    loss in Boraflex neutron absorption, and still maintain SFP B at less 
    than or equal to 0.95 k-effective when fully loaded and flooded with 
    unborated water. Florida Power Corporation has concluded that the 
    change in the criticality analysis methodology represents an unreviewed 
    safety question, and thus requires prior NRC approval.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        No. The two possible accidents are: (1) criticality during normal 
    storage and (2) criticality due to a misloaded fuel assembly during 
    handling fuel. Each are discussed below:
        (1) Criticality during normal storage.
        For criticality during normal storage to occur, there must be a 
    loss of negative reactivity since an addition of positive reactivity is 
    not possible without fuel movement. A loss in negative reactivity could 
    result only from reduction in Boraflex inventory below that needed to 
    meet the design basis. The proposed criticality analysis for Spent Fuel 
    Pool B demonstrates that Spent Fuel Pool B is capable of maintaining 
    the design basis requirement of k-effective less than or equal to 0.95 
    when flooded with unborated water and with a loss of up to 20% of the 
    Boraflex absorber material. Therefore, allowing up to 20% Boraflex loss 
    with the new analysis does not significantly increase the probability 
    of an accident previously evaluated.
        (2) Criticality during fuel handling.
        Criticality during fuel handling could occur due to loss of 
    negative reactivity, or the addition of positive reactivity. Loss of 
    negative reactivity could result from loss of Boraflex as discussed 
    above.
        Addition of positive reactivity would result from the misloading of 
    fuel in a fashion not in accordance with ITS LCO 3.7.15, such as the 
    misloading of a fresh 5.05% enriched fuel assembly into Region 2 or 
    side-by-side with another fresh fuel assembly in Region 1. The minimum 
    required boron concentration of ITS LCO 3.7.14 and CR-3 FSAR 9.3.2.1.2 
    are intended to compensate for just such an accident. Consistent with 
    the double-contingency principle, a boron dilution is not required to 
    be considered concurrent with a misloaded new fuel assembly (bases of 
    ITS LCO 3.7.14). The use of a new calculational method will not 
    increase the probability of fuel assembly misloading. A boron dilution 
    event without an accompanying misloaded fuel assembly is not impacted 
    by the new criticality analysis, since the design basis allows for 
    unborated water for normal storage conditions.
        Therefore, since the proposed criticality analysis does not 
    increase the probability of a misloaded fuel assembly, the probability 
    of an occurrence of an accident previously evaluated is not 
    significantly increased.
        Boraflex is credited with preventing inadvertent criticality. It is 
    not credited with mitigating the effects, or dose consequences, to the 
    public or to plant personnel from an inadvertent criticality. The 
    criticality analysis does not affect or mitigate the dose consequences 
    to the public or plant personnel from an inadvertent criticality.
        There are no other SAR accidents that could be affected. Therefore, 
    the use of the proposed criticality analysis, does not significantly 
    increase the consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        No. The only purpose, or function, of Boraflex is reactivity 
    control. Therefore, the use of the proposed criticality analysis can 
    only result in reactivity related accidents, such as an inadvertent 
    criticality. Though a spent fuel pool criticality accident is not 
    discussed in detail, a calculation to ensure such an accident could not 
    occur is referenced by both FSAR 9.3 and 9.6. Therefore, this is an 
    accident already discussed by the SAR and dependence on a new 
    criticality analysis does not create the possibility of an accident of 
    a new or different kind than any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        No. The proposed analysis demonstrates that the safety function and 
    design basis are met even for a Boraflex loss of up to 20%. Though the 
    proposed criticality analysis methodology is more realistic, and has 
    been licensed at other sites, it is less conservative than the 
    existing, NRC approved analysis that is currently part of the CR-3 
    licensing basis. Additionally, it permits operation with a greater loss 
    of Boraflex than the existing analysis.
        The current licensing basis, BAW-2209, ``Crystal River Unit 3 Spent 
    Fuel Storage Pool Criticality Analysis'', provides the analytical basis 
    of both ITS LCO 3.7.14 and LCO 3.7.15. This analysis uses very 
    conservative assumptions and methodologies, and results in very little 
    margin remaining for identified Boraflex loss. The margin of safety, 
    although less than previously evaluated, is not significantly reduced 
    with reliance on the current criticality analysis. The margin of safety 
    is restored with use of the proposed criticality analysis. Therefore, 
    the margin of safety is not significantly reduced with use of the 
    proposed criticality analysis.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
        Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC-A5A, P. O. Box 14042, St. Petersburg, Florida 
    33733-4042.
        NRC Project Director: Frederick J. Hebdon.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3 (CR-3), Citrus County, Florida
    
        Date of amendment request: November 23, 1998.
        Description of amendment request: The proposed amendment would 
    change the CR-3 Improved Technical Specifications (ITS) to raise the 
    Engineered Safeguards Actuation System (ESAS) setpoint for reactor 
    coolant system (RCS) low pressure from
    
    [[Page 71967]]
    
    1500 psig to 1625 psig. This change is intended to provide for earlier 
    actuation of high pressure injection (HPI) following certain small 
    break loss of coolant accidents and result in a lower peak center line 
    temperature (PCT) during these transients. The applicability 
    requirement for ESAS operability would be changed from greater than 
    1700 psig to greater than 1800 psig to maintain the previous margin 
    above the ESAS setpoint. Similarly, the reactor protection system (RPS) 
    setpoint for RCS low pressure and the RPS setpoint for Shutdown Bypass 
    (RCS High Pressure) would each be raised by 100 psig to maintain the 
    previous pressure margins. In addition, Surveillance Requirement 
    3.5.2.5 would be revised such that valves in the HPI flowpath that are 
    throttled to balance flow between the four HPI lines would be verified 
    in the correct position. The need for these changes resulted from 
    planned modifications to the HPI system to improve performance and 
    reliability of this system. Changes to ITS Bases necessitated by the 
    system modifications and setpoint changes are included in the 
    submittal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The setpoint changes for reactor trip and High Pressure Injection 
    (HPI) actuation will result in a very small (approximately one-percent) 
    increase in the probability for reactor trips. Review of industry data 
    shows that this increase is not significant. The revised accident 
    analysis has determined that transients which reduce Reactor Coolant 
    System (RCS) pressure below the new setpoints, warrant the associated 
    action. Engineered Safeguards Actuation System (ESAS) and Reactor 
    Protection System (RPS) actuations are used to mitigate accidents and 
    are not the initiator of analyzed accidents. Therefore, the probability 
    of previously evaluated accidents is not affected.
        RPS and ESAS functions are assumed to actuate to mitigate 
    transients. The revised setpoints will ensure earlier actuation of the 
    RPS and ESAS on a low RCS pressure condition. Raising the ESAS Low RCS 
    Pressure Setpoint will ensure earlier automatic HPI actuation for a 
    portion of the spectrum of pressure decreasing events. For rapid 
    depressurization events, such as main steam line break and large break 
    Loss of Coolant Accident (LOCA), this will have little impact. For 
    slower events, or those that do not reach the current setpoint during 
    the initial subcooled blowdown phase, HPI will be automatically 
    initiated substantially earlier in the event. This will increase the 
    integrated HPI flow to the RCS during the time the core is likely to be 
    uncovered, thereby reducing the consequential PCT. This additional flow 
    results in a significant peak clad temperature (PCT) decrease for small 
    break LOCA scenarios less than 0.07 square feet. Based on the above, 
    the consequences of previously evaluated accidents will not be 
    increased.
        The HPI system characteristics will not be affected such that the 
    probability of any accident is increased. The system flow restriction 
    for protection from low temperature overpressure (LTOP) events will be 
    maintained. The HPI system is used for accident mitigation and is not 
    the initiator of evaluated accidents other than LTOP. The proposed 
    surveillance changes will ensure that all valves throttled in the HPI 
    flowpath are verified and secured in the correct position. The throttle 
    valves and stop check valves will be positioned to ensure HPI flow is 
    within analyzed limits. Therefore, the consequences of accidents that 
    rely on HPI flow will not be increased.
        Based on the above evaluation, the probability or consequences of 
    evaluated accidents are not significantly increased by these changes.
        2. Does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The change to RPS and ESAS setpoints will not change the functions 
    of plant equipment, no new system interactions will be created, and no 
    new failure modes will be introduced. The setpoint changes will permit 
    earlier actuation for the associated actions. However, no new plant 
    conditions will be introduced by the setpoint changes.
        The HPI modifications include the installation of throttle valves 
    that will change the flow characteristics of the system. The new 
    throttle valves are manual valves that will be secured in position. The 
    revised surveillance requirements will ensure these valves are 
    positioned such that HPI flow is within analyzed limits. Therefore, no 
    conditions are created that could cause a new type of accident.
        Based on the above evaluation, these changes cannot create the 
    possibility of an accident of a different type than previously 
    evaluated in the [Safety Analysis Report] SAR.
        3. Does not involve a significant reduction in the margin of 
    safety.
        The safety function of the affected portions of the RPS and ESAS 
    systems is to actuate their respective functions if RCS pressure drops 
    below the setpoint. The raised RPS and ESAS setpoints will provide 
    earlier actuation for these protective features. These changes will 
    increase the margin of safety provided by the associated Technical 
    Specifications.
        The safety function of the HPI system is to provide cooling to 
    limit fuel peak clad temperature. The revised surveillance requirements 
    will ensure valves are positioned such that HPI flow is within analyzed 
    limits. Therefore, the margin of safety provided by the HPI 
    surveillance requirements is maintained.
        Based on the above evaluation, there is no reduction in the margin 
    of safety associated with the equipment and systems affected by this 
    change.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
        Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC--A5A, P. O. Box 14042, St. Petersburg, Florida 
    33733-4042.
        NRC Project Director: Frederick J. Hebdon.
    
    GPU Nuclear, Inc., et al., Docket No. 50-289, Three Mile Island Nuclear 
    Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: December 3, 1998.
        Description of amendment request: The proposed change revises the 
    TMI-1 Core Protection Safety Limits and Core Protection Safety Bases, 
    as specified in Technical Specification Figures 2.1-1 and 2.1-3, to 
    provide more restrictive limits which reflect the decrease in reactor 
    coolant system flow resulting from the analysis of increased once-
    through steam generator (OTSG) tube plugging limits (total allowable 
    number of tubes plugged). The licensee is currently restricted to a 
    total of 2,000 tubes plugged in both OTSGs which corresponds to 6.4 
    percent of the total number of tubes. The licensee's more restrictive 
    Core Protection Safety Limits reflect the reduction in reactor coolant
    
    [[Page 71968]]
    
    flow that would exist if an average of 20 percent of the OTSG tubes 
    were plugged.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the probability 
    of occurrence or the consequences of an accident previously evaluated. 
    An increase in the average steam generator tube plugging (SGTP) level 
    to 20% results in a small reduction of reactor coolant system (RCS) 
    flow rates and primary to secondary heat transfer. These changes result 
    in small changes to the primary and secondary side operating 
    parameters, and do not result in any additional challenges to plant 
    equipment. The proposed Technical Specification Changes resulting from 
    the increase in allowable tube plugging limits are more restrictive but 
    remain bounded by the existing reactor protection system (RPS) trip 
    setpoints. The assessment of the NSSS [nuclear steam supply system] 
    primary components, including the reactor pressure vessel, reactor 
    core, reactor coolant pump, steam generator, pressurizer, control rod 
    drive mechanisms, and RCS piping concluded that the integrity of these 
    components will be unaffected by the increase in average SGTP level.
        A re-analysis of the bounding Updated Final Safety Analysis Report 
    (UFSAR) Chapter 14 accidents, specifically the startup accident, loss 
    of coolant flow, loss of feedwater, and large and small break LOCA 
    demonstrated compliance with the acceptance criteria. The RCS pressure 
    boundary is not challenged, and the DNBR [departure from nucleate 
    boiling ratio] and peak clad temperature values remain within the 
    specified limits of the licensing basis. An analysis of the loss of 
    electric power accident demonstrated the ability of the plant to 
    transition smoothly to natural circulation with an average of 20% SGTP 
    or with asymmetric plugging. It was also determined that the current 
    mass and energy release data used for the containment integrity and 
    equipment qualification remain bounding. Since the design requirements 
    and safety limits continue to be met, system functions are not 
    adversely impacted, and the integrity of the RCS pressure boundary is 
    not challenged, the radiological consequences remain unchanged. 
    Therefore, this activity does not involve a significant increase in the 
    probability of occurrence or the consequences of an accident previously 
    evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different kind 
    of accident from any previously evaluated. The proposed Technical 
    Specification changes are more restrictive core protection safety 
    limits but remain bounded by the existing RPS trip setpoints. This 
    proposed change assures safe operation commensurate with the effects of 
    steam generator tube plugging. This increase in the average level of 
    SGTP to 20% will not introduce any new accident initiator mechanisms. 
    No new failure modes or limiting single failures have been identified. 
    Since the safety and design requirements continue to be met and the 
    integrity of the RCS pressure boundary is not challenged, no new 
    accident scenarios have been created. This change does not add any new 
    equipment, modify any interfaces with existing equipment, or change the 
    equipment function or the method of operating the equipment. Reactor 
    core, RCS, and steam generator parameters remain within appropriate 
    design limits during normal operation. Therefore, this activity does 
    not create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety. The existing RPS trip setpoints bound the proposed Technical 
    Specification changes resulting from 20% SGTP. This change assures safe 
    operation commensurate with the effects of steam generator tube 
    plugging. The TMI-1 DNB design basis, RCS pressure limits, peak clad 
    temperature limits and dose criteria are maintained for all UFSAR 
    transients. Therefore, this activity does not reduce the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania (REGIONAL DEPOSITORY), Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cecil O. Thomas.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2 (NMP2), Oswego County, New York
    
        Date of amendment request: November 16, 1998.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TSs) related to the implementation of 
    systems for the detection and suppression of coupled neutronic/thermal-
    hydraulic instabilities in the reactor. Average Power Range Monitor 
    (APRM) flow control trip reference cards will initiate a reactor scram 
    to limit the oscillation magnitude at reactor trip so as to limit the 
    associated Critical Power Ratio change and, in conjunction with Minimum 
    Critical Power Ratio (MCPR) operating limits, assure compliance with 
    the MCPR safety limit. In addition, the changes would increase the APRM 
    flow biased neutron flux scram and control rod block settings to allow 
    plant operation in the Extended Load Line Limit Analysis region. Thus, 
    the proposed changes are in regard to setpoints and calculations for 
    fuel cladding integrity and the associated TS Bases. In the Bases for 
    TS 2.1.1, the proposed change would reference new equations in TS 
    2.1.2a. In TS 2.1.2a, the proposed change would be to the equation for 
    determining the flow biased APRM scram and rod block trip setpoints. In 
    the Bases for TS 2.1.2a, the proposed change would reflect the new 
    setpoints. In the Bases for TS 2.2.2, the proposed change would be to 
    the description of the setpoint methodology which is based upon General 
    Electric Report NEDC-31336, ``GE Instrumentation Setpoint 
    Methodology.'' In Note (m) of TS Table 3.6.2/4.6.2, the proposed change 
    would be to the calibration range for the APRM channel setpoint. In the 
    Bases for TS 3.6.2/4.6.2, the proposed change would be to the equations 
    and methodology for determining APRM scram and rod block setpoints. In 
    TS 6.9.1.f, which identifies documents approved by NRC for analytical 
    methods used to determine core operating limits, the proposed change 
    would add ``NEDO-32465-A, Reactor Stability Detect and Suppress 
    Solutions Licensing Basis Methodology for Reload Applications, August 
    1996.''
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards
    
    [[Page 71969]]
    
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The APRM neutron monitoring system is not an initiator or a 
    precursor to an accident. The neutron monitoring system monitors the 
    power level of the reactor core and provides automatic core protection 
    signals in the event of a power transient. A Restricted Region will be 
    maintained such that the probability of a stability event is not 
    increased. Therefore, the proposed TS changes cannot affect the 
    probability of a previously evaluated accident.
        The proposed TS changes will revise the APRM flow-biased neutron 
    flux scram TS setting to provide automatic protection to assure that 
    anticipated coupled neutronic/thermal-hydraulic instabilities will not 
    compromise established fuel safety limits. The proposed changes will 
    result in a more restrictive APRM flow-biased scram trip setting in the 
    low flow regions of the power/flow operating map (i.e., operational 
    conditions where reactor instabilities are most probable). In other 
    words, the new settings will provide a scram sooner (at a lower power 
    level) than the existing settings. The associated control rod block 
    setting will also be revised. A margin between the control rod block 
    and flux scram has been determined by calculation.
        The proposed changes will also revise the APRM flow-biased neutron 
    flux scram and control rod block TS settings to provide an increase 
    above the current values in operating conditions not susceptible to 
    reactor instabilities. Specifically, the proposed changes will 
    implement a 2% increase in the analytical limit of the APRM flow-biased 
    flux scram and a 7% increase in the analytical limit of the APRM flow-
    biased control rod block. Evaluation demonstrates that these proposed 
    analytical limit increases have negligible impact on the transient 
    events results for NMP1 [Nine Mile Point Unit 1] as documented in 
    Chapter XV of the NMP1 UFSAR, [Updated Final Safety Analysis Report], 
    including the limiting transient events which are reanalyzed each 
    reload. Of the twenty-five (25) transient events analyzed in Section XV 
    of the NMP1 UFSAR, only the Inadvertent Startup of Cold Recirculation 
    Loop event and the Recirculation Flow Controller Malfunction--Increase 
    Flow event have potentially impacted results. The Chapter XV Control 
    Rod Drop Accident as well as the Turbine Trip with No Bypass at Partial 
    Power event were also evaluated.
        For the Inadvertent Startup of Cold Recirculation Loop event, the 
    proposed 2% increase in the high neutron flux scram would result in an 
    increase in the fuel average surface heat flux response. However, there 
    is significant margin between the surface heat flux value for this 
    event and the current limiting MCPR [Minimum Critical Power Ratio] 
    event (the Feedwater Controller Failure Maximum Demand event). As such, 
    any small change to the fuel surface heat flux response due to the high 
    neutron flux scram analytical limit increase would not result in the 
    fuel thermal margin requirements for the Inadvertent Startup of Cold 
    Recirculation Loop event to exceed the MCPR limits set by the limiting 
    reload analysis event.
        The reactor neutron flux for the Recirculation Flow Controller 
    Malfunction--Increase Flow event also showed an increasing trend from 
    its initial value. However, the peak response for this parameter (104% 
    of rated) is significantly below the high neutron flux scram analytical 
    limit. Accordingly, the proposed increase to the high neutron flux 
    scram analytical limit does not affect the response to this transient 
    event.
        The Control Rod Drop Accident is included in Chapter XV of the NMP1 
    UFSAR. As noted in NEDE-24011-P-A, ``GESTAR II: General Electric 
    Standard Application for Reactor Fuel,'' the initial power burst from 
    this event is terminated by the Doppler reactivity feedback while the 
    scram provides the final event termination several seconds later. The 
    120% APRM scram limit was conservatively chosen. The time delay 
    introduced by the small change in analytical limit will be 
    inconsequential due to the extremely rapid power rise for this event 
    (i.e., the time of scram for a 120% analytical limit vs. a 122% 
    analytical limit is essentially the same).
        The proposed Bases changes to TS 3.6.2/4.6.2 and TS 2.2.2 simply 
    provide details of the setpoint methodology currently used as well as 
    specific allowable values.
        Therefore, the proposed TS changes to implement a more restrictive 
    flow-biased scram setting to protect against reactor instabilities and 
    the proposed change to increase the high neutron flux scram and rod 
    block analytical limits do not result in a significant increase in the 
    consequences of an accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes will revise the APRM flow-biased neutron flux 
    scram TS settings to assure anticipated coupled neutronic/thermal-
    hydraulic instabilities will not compromise established fuel safety 
    limits in the low flow regions of the power/flow operating map as well 
    as revise the associated control rod block settings. These changes also 
    propose a 2% increase in the analytical limit of the APRM flow-biased 
    neutron flux scram and a 7% increase in the analytical limit of the 
    APRM flow-biased control rod block. These changes do not introduce any 
    new accident precursors and do not involve any alterations to plant 
    configurations which could initiate a new or different kind of 
    accident. The proposed changes do not affect the intended function of 
    the APRM system nor do they affect the operation of the system in a way 
    which would create a new or different kind of accident.
        Therefore, the proposed changes will not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        More conservative APRM flow-biased neutron flux scram and control 
    rod block settings will be implemented in the low flow regions of the 
    power/flow operating map. The scram setting change will assure that 
    anticipated coupled neutronic/thermal-hydraulic instabilities will not 
    compromise established fuel safety limits. The proposed changes will 
    also implement a 2% increase in the APRM flow-biased neutron flux scram 
    and a 7% increase in the APRM flow-biased control rod block in those 
    operating regions not susceptible to reactor instabilities. Evaluation 
    demonstrates that these proposed increases have negligible impact on 
    the transient events or accident results for NMP1. The impacted 
    transient events are either not the limiting MCPR event, the peak 
    response to the event is significantly below the high neutron flux 
    scram analytical limit or in the case of the Control Rod Drop Accident, 
    the time delay introduced by the change will be inconsequential due to 
    the extremely rapid power rise. No other events are adversely affected. 
    Therefore, the proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this
    
    [[Page 71970]]
    
    review, it appears that the three standards of 50.92(c) are satisfied. 
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2 (NMP2), Oswego County, New York
    
        Date of amendment request: November 19, 1998.
        Description of amendment request: The proposed amendment would 
    change the surveillance frequencies in Technical Specifications (TSs) 
    4.8.4.4a, ``Surveillance Requirements--Reactor Protection System 
    Electric Power Monitoring (RPS Logic),'' and 4.8.4.5a, ``Surveillance 
    Requirements--Reactor Protection System Electric Power Monitoring 
    (Scram Solenoids),'' to require channel functional testing of the RPS 
    Motor Generator Set (M/G) and RPS Uninterruptible Power Supplies (UPS) 
    Electrical Protection Assemblies (EPAs) at least once every 6 months. 
    These TSs currently require that channel functional testing be 
    performed each time the plant is in cold shutdown for a period of more 
    than 24 hours, unless performed within the previous 6 months.
        Basis for proposed no significant hazards consideration 
    determination: During the last refueling outage, the licensee modified 
    the Nine Mile Point Unit No. 2 (NMP2) design for the RPS M/G and RPS 
    UPS EPAs to provide relay actuated protection systems. The relays of 
    the new design may be individually isolated from an essential power 
    circuit for testing and may be actuated without tripping the associated 
    breaker. The relay actuated system will allow the EPA system monitoring 
    an essential power supply to be functionally tested with the plant on-
    line. The EPA relay actuation setpoints are not affected by the 
    modification or the proposed TS changes. The licensee states that the 
    design, installation, and testing of the new units meet the criteria of 
    the same standards that were applied to the previous units.
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes affect surveillance testing frequency only. 
    The new relay actuated protection system design functions in the same 
    fail safe manner as the old units. Also, the new design in conjunction 
    with the testing capability has increased EPA reliability, while 
    introducing little risk to testing the EPAs with the plant in 
    operation. Therefore, the proposed changes to the NMP2 TS do not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes affect surveillance testing frequency of relay 
    actuated protection circuits only. The proposed changes do not 
    introduce any new or different accident initiators from any that were 
    previously evaluated. EPA relay actuation setpoints are not affected. 
    The actual fail safe system conditions required for EPA actuation will 
    remain the same. Therefore, the operation of NMP2, in accordance with 
    the proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The function of the EPA systems is to isolate the loads from supply 
    power. That function was not altered by the proposed change. 
    Reliability of the EPA systems is improved. Therefore, the operation of 
    NMP2, in accordance with the proposed amendment, will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station, Unit 1 (NMP1), Oswego County, New York
    
        Date of amendment request: November 30, 1998.
        Description of amendment request: The proposed amendment would 
    correct Technical Specification (TS) 3.1.2, ``Liquid Poison System,'' 
    and the associated TS Bases. Specifically, in the Bases for TS 3.1.2, 
    the boron-10 concentration of 120 ppm (which is incorrectly calculated 
    using atomic percent instead of weight percent) would be changed to 
    109.8 ppm. In TS 3.1.2, the minimum volume of the sodium pentaborate 
    solution contained in the Liquid Poison System storage tank would be 
    increased from 1185 gallons to 1325 gallons.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The Liquid Poison System is designed to provide the capability to 
    bring the reactor from a full design rating to a shutdown condition 
    assuming none of the control rods can be inserted. The system is 
    manually initiated in response to a failure of the Control Rod Drive 
    System to shutdown the reactor. The proposed changes revise the 
    required liquid poison solution volume and concentration. The proposed 
    changes to the Technical Specifications and the Bases require no 
    changes to the physical facility which could adversely affect any 
    accident precursors. Therefore, the proposed changes cannot 
    significantly increase the probability of an accident.
        The proposed changes will assure that the Liquid Poison System 
    continues to provide the capability to shutdown the reactor during an 
    ATWS [Anticipated Transient Without Scram] event. In addition, the 
    system will continue to be capable of bringing the reactor to cold 
    shutdown, 3 percent delta k subcritical (0.97 keff), from a 
    full design rating of
    
    [[Page 71971]]
    
    1850 megawatts thermal assuming none of the control rods can be 
    inserted, and considering the combined effects of coolant voids, 
    temperature change, fuel doppler, and xenon and samarium. Therefore, 
    the change to the Technical Specifications does not significantly 
    increase the consequences of a previously evaluated accident.
        2. The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Injection of the sodium pentaborate solution into the reactor 
    vessel has been considered in the plant design. The proposed changes 
    revise the required liquid poison solution volume and concentration. 
    The proposed changes make no physical modification to the plant which 
    could create the possibility of a new or different kind of accident. 
    The proposed changes will maintain the capability of the Liquid Poison 
    System to shutdown the reactor from its full design rating assuming 
    none of the control rods are inserted, and considering the combined 
    effects of coolant voids, temperature change, fuel doppler, and xenon 
    and samarium. Consequently, these changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed changes revise the required liquid poison solution 
    volume and concentration. The proposed changes make no physical 
    modification to the plant which could reduce the margin of safety. 
    These changes will assure compliance with the requirements of 
    10CFR50.62, ``Requirements for Reduction of Risk from Anticipated 
    Transients without Scram (ATWS) Events for Light-Water-Cooled Nuclear 
    Power Plants.'' In addition, these changes will maintain the capability 
    of the Liquid Poison System to bring the reactor from a full design 
    rating of 1850 megawatts thermal to greater than 3 percent delta k 
    subcritical (0.97 keff) assuming none of the control rods 
    can be inserted, and considering the combined effects of coolant voids, 
    temperature change, fuel doppler, xenon and samarium.
        The required volume of boron-10 solution in the Liquid Poison 
    System storage tank includes an additional 25 percent margin beyond the 
    amount needed to shutdown the reactor to allow for any unexpected non-
    uniform mixing. Also, the total storage tank volume of sodium 
    pentaborate solution incorporates 197 gallons of solution which is 
    unavailable for injection into the reactor vessel and a 25 gallon 
    margin for conservatism. Additionally, using one 30 gpm Liquid Poison 
    System pump, the injection time is greater than 17 minutes thereby 
    assuring adequate mixing. The proposed changes to the liquid poison 
    concentration and volume ensure the NMP1 [Nine Mile Point Unit 1] 
    Liquid Poison System is able to meet its safety function requirements. 
    Therefore, this change will not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa.
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: December 4, 1998.
        Description of amendment request: The proposed amendment would 
    eliminate the need to cycle the plant and its components through a 
    shutdown-startup cycle by allowing the next snubber surveillance 
    interval to be deferred until the end of refueling outage 6 or 
    September 10, 1999, whichever date is earlier.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 10 CFR 
    50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this conclusion 
    is that the three criteria of 10CFR50.92(c) are not satisfied. The 
    proposed revision does not involve [an] SHC because the revision would 
    not:
        1. Involve a significant increase in the probability or consequence 
    of an accident previously evaluated.
        The proposed change is for a one time extension to the surveillance 
    interval of snubber inspections required by Technical Specification 
    4.7.10.e. The change involves revising the calendar time for snubber 
    interval inspections to 36 months to coincide with the time frame of 
    the current cycle 6 operation.
        Snubber testing experience at Millstone Unit No. 3 has shown that 
    historical failure rates of snubbers are low. During the third 
    refueling outage, after an operating cycle of approximately 22 months, 
    the functional testing program identified multiple Type A failures 
    attributed primarily to original plant construction, and resulted in a 
    full inspection of all Type A snubbers. The snubber inspection interval 
    was extended to approximately 30 months by a one-time extension to the 
    Technical Specifications for the fourth refueling outage and only one 
    Type A snubber failure was identified. Subsequent outages with 
    operating durations of 18 and 17 months also identified only a single 
    Type B failure in each outage. The results of piping stress analysis 
    which have been performed to assess the impact of snubbers which have 
    failed to meet functional test acceptance criteria have shown that 
    neither piping system functionality or structural integrity have ever 
    been compromised.
        During the recent cycle 6 operation Millstone 3 has experienced an 
    extended midcycle shutdown, where temperature, vibration effects and 
    normal wear on snubbers have been minimized as compared to a normal 
    operating cycle. The last snubber surveillance interval inspections 
    were completed during this midcycle shutdown. Although the calendar 
    surveillance interval is impacted by this change the primary conditions 
    that present challenges to snubbers have not been prevalent during the 
    extended shutdown. Given the low failure rates of snubbers over the 
    last 3 surveillance intervals, and the fact the operating time of the 
    remainder of cycle 6 will be approximately 1 year, snubber failures are 
    expected to be similar to previous intervals.
        Accordingly the possibility of a snubber failure leading to a 
    Decrease in Reactor Coolant Inventory or a Decrease in Heat Removal by 
    the Secondary System is not increased and there is no affect on the 
    probability of previously evaluated accidents.
        This change does not include any physical changes to the plant and 
    does not affect acceptance criteria or the
    
    [[Page 71972]]
    
    required actions for functional failures of snubbers. Accordingly there 
    is no increase in the consequences of previously evaluated accidents 
    resulting in a Decrease in Reactor Coolant Inventory or a Decrease in 
    Heat Removal by the Secondary System.
        Thus it is concluded that the proposed revision does not involve a 
    significant increase in the probability or consequence of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        This proposed revision to the surveillance interval does not change 
    the operation of any plant system or component during normal or 
    accident conditions. The proposed change extends the surveillance 
    interval of snubber inspections required by Technical Specification 
    4.7.10.e. The change involves revising the calendar time for snubber 
    interval inspections to coincide with the time frame of current cycle 6 
    operation. This change does not include any physical changes to the 
    plant and does not affect acceptance criteria or the required actions 
    for functional failures of snubbers.
        Thus, this proposed revision does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change extends the surveillance interval of snubber 
    inspections required by Technical Specification 4.7.10.e. The change 
    involves revising the calendar time for snubber interval inspections to 
    coincide with the time frame of current cycle 6 operation. This change 
    does not include any physical changes to the plant and does not affect 
    acceptance criteria or the required actions for functional failures of 
    snubbers. The service life of the snubbers or parts as required by 
    Technical Specification 4.7.10.i will not be impacted by this change 
    since the required replacements have already occurred and no additional 
    service life dates will expire prior to September 10, 1999.
        Thus, it is concluded that the proposed revision does not involve a 
    significant reduction in a margin of safety.
        In conclusion, based on the information provided, it is determined 
    that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, Attn: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    Connecticut.
        NRC Project Director: William M. Dean.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. Ginna 
    Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: November 24, 1998.
        Description of amendment request: The proposed amendment would 
    revise the Ginna Station Improved Technical Specifications description 
    of the fuel cladding material (TS 4.2.1) and to update the list of 
    references provided in Specification 5.6.5 for the Core Operating 
    Limits Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Evaluation of Administrative Changes
    
        The administrative changes [related to the update of references 
    provided in Specification 5.6.5 for the Core Operating Limits report] 
    do not involve a significant hazards consideration as discussed below:
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The proposed changes 
    revise Administrative Controls Section 5.6.5.b to update the references 
    to NRC approved documents which support the analysis for the Heat Flux 
    Hot Channel Factor in the Core Operating Limits Report and to provide 
    clarification to the currently applicable methodology. It revises the 
    Design Features Section 4.2.1 to provide clarification of the types of 
    zirconium alloy filler rod material that have received previous NRC 
    approval and to clarify that the application shall be NRC approved. 
    Section 4.2.1 is revised to clarify that the analyses performed to 
    verify compliance with the fuel safety design bases shall be cycle 
    specific. As such, these changes are administrative in nature and do 
    not impact initiators or analyzed events or assumed mitigation of 
    accident or transient events. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an accident 
    previously analyzed.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The proposed 
    administrative changes do not affect the manner by which the plant is 
    operated and no new equipment will be installed. The proposed 
    administrative changes will not impose any new or different 
    requirements. All original design and performance criteria continue to 
    be met, and no new failure modes have been created for any system, 
    component, or piece of equipment. Thus, these changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of safety. 
    The proposed changes will not reduce a margin of plant safety because 
    the methodology has been shown to meet all applicable design criteria 
    and ensure that all pertinent licensing basis acceptance criteria are 
    met. As such, no question of safety is involved, and the changes do not 
    involve a significant reduction in a margin of safety.
    
    Evaluation of Less Restrictive Changes
    
        The less restrictive change [related to the fuel cladding material 
    (TS 4.2.1)] does not involve a significant hazards consideration as 
    discussed below:
        (1) Operation of Ginna Station in accordance with the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The Westinghouse 
    14 x 14 VANTAGE + fuel assemblies containing fuel rods fabricated with 
    ZIRLO alloy meet the same fuel assembly and fuel rod design bases as 
    Westinghouse 14 x 14 OFA [Optimized Fuel Assembly] fuel assemblies in 
    the other fuel regions. In addition, the 10 CFR 50.46 criteria will be 
    applied to the fuel rods fabricated with ZIRLO alloy. The use of these 
    fuel assemblies will not result in a change to the proposed Ginna 
    Westinghouse 14 x 14 OFA reload design and safety analysis limits. The 
    ZIRLO alloy is similar in chemical composition and has similar physical 
    and mechanical properties as that of Zircaloy-4. Thus the cladding 
    integrity is maintained and the structural integrity of the fuel
    
    [[Page 71973]]
    
    assembly is not affected. The ZIRLO clad fuel rods improve corrosion 
    resistance and dimensional stability. The use of ZIRLO does not impact 
    the radiological consequences of accidents previously evaluated in the 
    Safety Analysis. The RCS [reactor coolant system] isotopic inventory is 
    negligibly impacted; therefore, changes in postulated releases from the 
    RCS or the secondary systems are negligible. Assumptions of fuel 
    melting in the radiological analyses are not based on the type of fuel 
    cladding. For those accidents where fuel melting is postulated to occur 
    (control rod ejection, locked [seized] RCP rotor), the amount of fuel 
    undergoing melting and clad damage using ZIRLO clad is bounded by the 
    current values used in the Safety Analysis. Therefore, the probability 
    or consequences of an accident previously evaluated is not 
    significantly increased.
        (2) Operation of Ginna Station in accordance with the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The Westinghouse 
    14 x 14 VANTAGE + fuel assemblies containing fuel rods fabricated with 
    ZIRLO alloy will satisfy the same design bases as that used for 
    Westinghouse 14 x 14 OFA fuel assemblies in the other fuel regions. 
    Since the original design criteria is being met, the fuel rods 
    fabricated with ZIRLO alloy will not be an initiator for any new 
    accident. All design and performance criteria will continue to be met 
    and no new single failure mechanisms have been created. In addition, 
    the use of these fuel assemblies does not involve any alterations to 
    plant equipment or procedures which would introduce any new or unique 
    operational modes or accident precursors. Therefore, the possibility 
    for a new or different kind of accident from any accident previously 
    evaluated is not created.
        (3) Operation of Ginna Station in accordance with the proposed 
    change does not involve a significant reduction in a margin of safety. 
    The Westinghouse 14 x 14 VANTAGE + fuel assemblies containing fuel rods 
    fabricated with ZIRLO alloy do not change the proposed Ginna 
    Westinghouse 14 x 14 OFA reload design and safety analysis limits. The 
    use of these fuel assemblies containing fuel rods fabricated with ZIRLO 
    alloy will take into consideration the normal core operating conditions 
    allowed in the Technical Specifications. For each cycle reload core, 
    these fuel assemblies will be specifically evaluated using approved 
    reload design methods and approved fuel rod design models and methods 
    as specified in Technical Specifications. This will include 
    consideration of the core physics analysis peaking factors and core 
    average linear heat rate effects. In addition, the 10 CFR 50.46 
    criteria will be applied each cycle to the fuel rods fabricated with 
    ZIRLO alloy. Analyses or evaluations will be performed each cycle to 
    confirm that 10 CFR 50.46 will be met. Therefore, the margin of safety 
    as defined in the Bases to the Ginna Technical Specifications is not 
    significantly reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005.
        NRC Project Director: S. Singh Bajwa.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362,
    
    San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California
    
        Date of amendment requests: November 23, 1998.
        Description of amendment requests: The proposed change would revise 
    the Technical Specifications (TS) to (1) reinstate the log power 
    reactor trip at or above 4E-5% RATED THERMAL POWER (RTP); (2) reinstate 
    reactor trips for Reactor Coolant Flow--Low (RCS flow), the Local Power 
    Density--High (LPD), and the Departure from Nucleate Boiling Ratio--Low 
    (DNBR); (3) remove the word ``automatically'' from notes (a) and (d) of 
    Table 3.3.1-1 to clarify that the manual enable of the trip is 
    permissible; and, (4) clarify that the setpoints on Table 3.3.1-1 are 
    set relative to logarithmic power, not thermal power.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change to TS 3.3.1 does not adversely impact 
    structure, system, or component design or operation in a manner which 
    would result in a change in the frequency of occurrence of accident 
    initiation. SCE has re-analyzed the relevant accidents and established 
    that accident consequences are not significantly increased by the 
    proposed changes to the bypass-permissive and enable setpoints. The 
    reactor trip bypass and automatic enable functions are not accident 
    initiators. Consequently, the proposed TS change will not significantly 
    increase the probability of accidents previously evaluated. Therefore, 
    this amendment request does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        No new or different accidents result from changing the reactor trip 
    bypass-permissive and automatic enable setpoints. Introducing an 
    uncertainty band for the enable setpoints delays the mitigation action 
    of the reactor trip for the design basis analysis for the events that 
    credit this trip. The enable setpoint itself does not cause any 
    accident. Therefore, the amendment request does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        SCE [Southern California Edison Company] has re-analyzed the 
    accidents and determined that the consequences of the accidents are 
    within their acceptance criteria under the proposed amendment so that 
    the margin of safety that bounds the setpoint in both directions 
    remains intact. The analyses are relatively insensitive to the reactor 
    trip automatic enable setpoints, and no significant reduction in the 
    margins of safety ensues from the relatively minor proposed changes to 
    the bypass-permissive and enable setpoints, nor from establishing 
    allowable values for these points.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: Douglas K. Porter, Esquire, Southern 
    California Edison Company, P.O. Box 800, Rosemead, California 91770.
    
    [[Page 71974]]
    
        NRC Project Director: William H. Bateman.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: November 23, 1998.
        Description of amendment request: The proposed amendment relocates 
    descriptive design information from Technical Specification 3/4.7.1.1 
    (Table 3.7-2), regarding orifice sizes for main steam line Code safety 
    valves, to the Bases section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change relocates the orifice size design information 
    for the main steam line Code safety valves, found in Table 3.7-2, that 
    does not meet the criteria for inclusion in Technical Specifications as 
    identified in 10 CFR 50.36(c)(2)(ii). The affected descriptive design 
    information is not related to any assumed initiators of analyzed events 
    and is not assumed to mitigate accident or transient events. The 
    limiting condition for operation for the main steam line Code safety 
    valves is not altered by the proposed change. The orifice size design 
    information will be relocated from Table 3.7-2 of Specification 3/
    4.7.1.1 to the Bases section for that same Technical Specification and 
    will be maintained pursuant to 10 CFR 50.59. In addition, surveillance 
    testing details for this Technical Specification are addressed in 
    existing surveillance procedures, which are also controlled by 10 CFR 
    50.59, and subject to the change control provisions imposed by plant 
    administrative procedures, which endorse applicable regulations and 
    standards. Therefore, the change does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change relocates the orifice size design information 
    for the main steam line Code safety valves, found in Table 3.7-2, that 
    does not meet the criteria for inclusion in Technical Specifications as 
    identified in 10 CFR 50.36(c)(2)(ii). The change does not involve a 
    physical alteration of the plant (no new or different type of equipment 
    will be installed) or make changes in the methods governing normal 
    plant operation. The change will not impose different requirements, and 
    adequate control of information will be maintained. This change will 
    not alter assumptions made in the safety analysis and licensing basis. 
    Therefore, the change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed change relocates the orifice size design information 
    for the main steam line Code safety valves, found in Table 3.7-2, that 
    does not meet the criteria for inclusion in Technical Specifications as 
    identified in 10 CFR 50.36(c)(2)(ii). The change will not reduce a 
    margin of safety since it has no impact on any safety analysis 
    assumptions. In addition, the relocated orifice size design information 
    remains the same as the existing Technical Specifications. Since any 
    future changes to this orifice size information (that will be located 
    in the Bases section) will be evaluated per the requirements of 10 CFR 
    50.59, there is no reduction in a margin of safety.
        The proposed change is also consistent with the Westinghouse Plants 
    (Improved) Standard Technical Specification, NUREG-1431, approved by 
    the NRC Staff. Revising the Technical Specification to reflect the 
    approved content of NUREG-1431 ensures no significant reduction in the 
    margin of safety. Therefore, the change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869.
        NRC Project Director: John N. Hannon.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: November 11, 1998.
        Brief description of amendments: The proposed amendments revise 
    core safety limit curves and Overtemperature N-16 reactor trip 
    setpoints based on analyses of the core configuration and expected 
    operation for Comanche Peak Steam Electric Station (CPSES) Unit 2, 
    Cycle 5. The changes apply equally to CPSES Units 1 and 2 licenses 
    since the Technical Specifications are combined.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        A. Revision to the Unit 2 Core Safety Limits
        Analyses of reactor core safety limits are required as part of 
    reload calculations for each cycle. TU Electric has performed the 
    analyses of the Unit 2, Cycle 5 core configuration to determine the 
    reactor core safety limits. The methodologies and safety analysis 
    values result in new operating curves which, in general, permit plant 
    operation over a similar range of acceptable conditions. This change 
    means that if a transient were to occur with the plant operating at the 
    limits of the new curve, a different temperature and power level might 
    be attained than if the plant were operating within the bounds of the 
    old curves. However, since the new curves were developed using NRC 
    approved methodologies which are wholly consistent with and do not 
    represent a change in the Technical Specification BASES for safety 
    limits, all applicable postulated transients will continue to be 
    properly mitigated. As a result, there will be no significant increase 
    in the consequences, as determined by accident analyses, of any 
    accident previously evaluated.
        B. Revision to Unit 2 Overtemperature N-16 Reactor Trip Setpoints
        As a result of changes discussed, the Overtemperature reactor trip 
    setpoint has been recalculated. These trip setpoints help ensure that 
    the core safety limits are protected and that all applicable limits of 
    the safety analysis are met.
        Based on the calculations performed, no significant changes to the 
    safety
    
    [[Page 71975]]
    
    analysis values for Overtemperature reactor trip setpoint were 
    required. The f(delta I) trip reset function was revised due to less 
    top-skewed axial power distributions predicted for this cycle. The 
    analyses performed show that, using the TU Electric methodologies, all 
    applicable limits of the safety analysis are met. This setpoint 
    provides a trip function which allows the mitigation of postulated 
    accidents and has no impact on accident initiation. Therefore, the 
    changes in safety analysis values do not involve an increase in the 
    probability of an accident and, based on satisfying all applicable 
    safety analysis limits, there is no significant increase in the 
    consequences of any accident previously evaluated.
        In addition, sufficient operating margin has been maintained in the 
    overtemperature setpoint such that the risk of turbine runbacks or 
    unnecessary reactor trips due to upper plenum flow anomalies or other 
    operational transients will be minimized, thereby, reducing potential 
    challenges to the plant safety systems.
        C. Administrative changes to reflect plant nomenclature
        Changes to the N-16 trip setpoint equation are for clarification 
    only to more accurately reflect CPSES plant nomenclature. This change 
    is administrative in nature and does not increase in the probability or 
    consequences of an accident previously evaluated.
    
    Summary
    
        The changes in the amendment request apply NRC approved 
    methodologies to changes in safety analysis values, new core safety 
    limits and new N-16 setpoint and parameter values to assure that all 
    applicable safety analysis limits have been met. The potential for an 
    operational transient to occur has not been affected and there has been 
    no significant impact on the consequences of any accident previously 
    evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed changes involve the calculation of new reactor core 
    safety limits and overtemperature reactor trip setpoint resets. As 
    such, the changes play an important role in the analysis of postulated 
    accidents but none of the changes effect plant hardware or the 
    operation of plant systems in a way that could initiate an accident. 
    Changes to the N-16 trip setpoint equation are for clarification only 
    to more accurately reflect CPSES plant nomenclature. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        In reviewing and approving the methods used for safety analyses and 
    calculations, the NRC has approved the safety analysis limits which 
    establish the margin of safety to be maintained. While the actual 
    impact on safety is discussed in response to question 1, the impact on 
    margin of safety is discussed below:
        A. Revision to the Unit 2 Reactor Core Safety Limits
        The NRC-approved TU Electric reload analysis methods have been used 
    to determine new reactor core safety limits. All applicable safety 
    analysis limits have been met. The methods used are wholly consistent 
    with Technical Specification BASES 2.1 which is the bases for the 
    safety limits. In particular, the curves assure that for Unit 2, Cycle 
    5, the calculated DNBR is no less than the safety analysis limit and 
    the average enthalpy at the vessel exit is less than the enthalpy of 
    saturated liquid. The acceptance criteria remains valid and continues 
    to be satisfied; therefore, no change in a margin of safety occurs.
        B. Revision to Unit 2 Overtemperature N-16 Reactor Trip Setpoints
        Because the reactor core safety limits for CPSES Unit 2, Cycle 5 
    are recalculated, the Reactor Trip System instrumentation setpoint 
    values for the Overtemperature N-16 reactor trip setpoint which protect 
    the reactor core safety limits must also be recalculated. The 
    Overtemperature N-16 reactor trip setpoint helps prevent the core and 
    Reactor Coolant System from exceeding their safety limits during normal 
    operation and design basis anticipated operational occurrences. The 
    most relevant design basis analysis in Chapter 15 of the CPSES Final 
    Safety Analysis Report (FSAR) which is affected by the Overtemperature 
    reactor trip setpoint is the Uncontrolled Rod Cluster Control Assembly 
    Bank Withdrawal at Power (FSAR Section 15.4.2). This event has been 
    analyzed with the new safety analysis value for the Overtemperature 
    reactor trip setpoint to demonstrate compliance with event specific 
    acceptance criteria. Because all event acceptance criteria are 
    satisfied, there is no degradation in a margin of safety.
        The nominal Reactor Trip System instrumentation setpoint values for 
    the Overtemperature N-16 reactor trip setpoint (Technical Specification 
    Table 2.2-1) are determined based on a statistical combination of all 
    of the uncertainties in the channels to arrive at a total uncertainty. 
    The total uncertainty plus additional margin is applied in a 
    conservative direction to the safety analysis trip setpoint value to 
    arrive at the nominal and allowable values presented in Technical 
    Specification Table 2.2-1. Meeting the requirements of Technical 
    Specification Table 2.2-1 assures that the Overtemperature reactor trip 
    setpoint assumed in the safety analyses remains valid. The CPSES Unit 
    2, Cycle 5 Overtemperature reactor trip setpoint is not significantly 
    different from the previous cycle, and thus provides operational 
    flexibility to withstand mild transients without initiating automatic 
    protective actions. Although the value of the f(delta I) trip reset 
    function setpoint is different, the Reactor Trip System instrumentation 
    setpoint values for the Overtemperature N-16 reactor trip setpoint are 
    consistent with the safety analysis assumptions which have been 
    analytically demonstrated to be adequate to meet the applicable event 
    acceptance criteria. Thus, there is no reduction in a margin of safety.
        Using the NRC approved TU Electric methods, the reactor core safety 
    limits are determined such that all applicable limits of the safety 
    analyses are met. Because the applicable event acceptance criteria 
    continue to be met, there is no significant reduction in the margin of 
    safety.
        C. Administrative changes to reflect plant nomenclature
        Changes to the N-16 trip setpoint equation are for clarification 
    only to more accurately reflect CPSES plant nomenclature. This change 
    is administrative in nature and has no impact on the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019.
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036.
        NRC Project Director: John N. Hannon.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: December 10, 1998.
    
    [[Page 71976]]
    
        Description of amendment request: The licensee proposed to correct 
    an error in the technical specifications by changing to the use of 
    ``hydrogen, balance air'' rather than the incorrect ``hydrogen balance 
    nitrogen'' for calibration of the Augmented Offgass System hydrogen 
    monitors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        Based on the criteria for defining a significant hazards 
    consideration in 10CFR50.92, operation of VYNPS in accordance with this 
    change would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:
        The proposed change is purely administrative in nature--correcting 
    instrument calibration requirements to conform the Technical 
    Specification with the instrument manufacturer's recommendations. The 
    change has no effect on plant hardware, plant design, safety limit 
    setting, or plant system operation and therefore does not modify or add 
    any initiating parameters that would significantly increase the 
    probability or consequences of an accident previously evaluated. This 
    change to the Technical Specifications is a correction of an error 
    which occurred when the particular Technical Specification was issued. 
    The function of this surveillance requirement remains unchanged.
        No new modes of operation are introduced by the proposed change 
    such that adverse consequences would result. Accordingly, the 
    consequences of previously analyzed accidents are not affected by this 
    proposed change.
        The Augmented Off-Gas (AOG) System hydrogen monitors do not serve a 
    reactor safety function. In this context, the determination of no 
    significant hazards consideration defined in 10CFR50.92 is made based 
    on the ``accident previously evaluated'' being a postulated hydrogen 
    detonation within the off-gas system downstream of the hydrogen 
    recombiners. The hydrogen monitors do not mitigate the consequences of 
    an accident, but rather function to preclude a hydrogen explosion 
    within the off-gas system. The function of the Augmented Off-Gas System 
    hydrogen monitors to prevent a hydrogen detonation is not affected by 
    this change.
        (2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated, because:
        Since this change merely corrects Technical Specification wording 
    to reflect the actual manufacturer's recommended gas mixture to be used 
    for calibrating these instruments, no new or different types of 
    accidents are created. Since the calibration gas mixture has a very low 
    (approximately 2%) hydrogen concentration, its use does not introduce 
    the possibility of fires, explosions, or other hazards which might 
    adversely affect safety-related equipment. Therefore, use of the proper 
    calibration gas does not create the possibility of a new or different 
    kind of accident.
        This change does not affect the operation of any systems or 
    components, nor does it involve any potential initiating events that 
    would create any new or different kind of accident. Therefore, the 
    proposed change does not create the possibility of a new or different 
    kind of accident from any previously evaluated for the Vermont Yankee 
    Nuclear Power Station.
        (3) Involve a significant reduction in a margin of safety, because:
        This proposed change involving the specification of the correct 
    calibration gas mixture ensures that the off-gas system hydrogen 
    monitors are properly calibrated and therefore preserve the margin of 
    safety in precluding a hydrogen explosion in the off-gas system. 
    Administratively changing this specification only establishes the 
    appropriate calibration gas for the actual, installed hydrogen 
    monitors. Changing the specification to reflect correct practice will 
    not reduce the margin of safety.
        The proposed change does not affect any equipment involved in 
    potential initiating events or safety limits. Therefore, it is 
    concluded that the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Project Director: Cecil O. Thomas.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: July 30, 1998 (TSCR 206).
        Description of amendment request: The purpose of the proposed 
    amendments is to incorporate changes to the Technical Specifications to 
    more clearly define the requirements for Service Water (SW) System 
    operability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendment[s] does not result in a significant increase in 
    the probability or consequences of any accident previously evaluated.
        The Service Water System is primarily a support system for systems 
    required to be operable for accident mitigation. Portions of the SW 
    system supplying the containment fan coolers also function as part of 
    the containment pressure boundary under post accident conditions. 
    Failures within the SW system are not an initiating condition for any 
    analyzed accident.
        Analyses performed demonstrate that under the Technical 
    Specifications allowable configurations, the SW system will continue to 
    perform all required functions. The SW system is capable of supplying 
    the required cooling water flow to systems required for accident 
    mitigation. That is, the SW system removes the required heat from the 
    containment fan coolers and residual heat removal heat exchangers 
    ensuring containment pressure and temperature profiles following an 
    accident are as evaluated in the FSAR [final safety analysis report]. 
    This in turn ensures that environmental qualification of equipment 
    inside containment is maintained and thus function as required post-
    accident.
        SW system response post accident is within all design limits for 
    the system. Transient and steady state forces within the system remain 
    within all design and operability limits thereby maintaining the 
    integrity of the system inside containment and the integrity of the 
    containment pressure boundary. Assumptions dependent on containment 
    pressure profile for containment leakage assumed in the radiological 
    consequence analyses remain valid.
        In addition, removing required heat from containment ensures that 
    cooling
    
    [[Page 71977]]
    
    of the reactor core is accomplished for long-term accident mitigation.
        Therefore, operation of the SW system as proposed will not result 
    in a significant increase in the probability or consequences of any 
    accident previously evaluated.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not result in a new or different kind of 
    accident from any accident previously evaluated.
        The proposed changes do not alter the way in which the SW system 
    performs its design functions nor the design limits of the system. The 
    proposed changes do not introduce any new or different normal operation 
    or accident mitigation functions for the system. Therefore, no new 
    accident initiators are introduced by the proposed changes. Operation 
    of SW system as proposed cannot result in a new or different kind of 
    accident from any accident previously evaluated.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not result in a significant reduction in a 
    margin of safety.
        Analyses performed in support of the proposed amendments 
    demonstrate that the SW system continues to perform its function as 
    assumed and credited in the accident analyses and radiological 
    consequence analyses performed for the Point Beach Nuclear Plant. 
    Therefore, the analyses and results are not changed. All analysis 
    limits remain met. The SW system continues to be operated and responds 
    within all design limits for the system. Therefore, operation of the 
    Point Beach Nuclear Plant in accordance with the proposed amendments 
    cannot result in a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: September 23, 1998 (TSCR 209).
        Description of amendment request: The purpose of the proposed 
    amendments is to remove the test requirements for snubbers from the 
    Technical Specifications (TS). These requirements are already included 
    in the Point Beach Nuclear Plant In-Service Inspection Program.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not result in a significant increase in 
    the probability or consequences of an accident previously evaluated.
        These changes do not involve a significant increase in the 
    probability of an accident previously evaluated because no such 
    accidents are affected by the proposed revisions to delete TS 15.4.3. 
    The proposed TS change does not introduce any new accident initiators.
        Initiating conditions and assumptions are unchanged and remain as 
    previously analyzed for accidents in the PBNP Final Safety Analysis 
    Report. The proposed TS change does not involve any physical changes to 
    systems or components, nor does it alter the typical manner in which 
    the systems or components are operated. Therefore, these changes do not 
    increase the probability of previously evaluated accidents.
        As noted above, the snubber testing requirements included in the 
    ASME/ANSI OM-4 Code are more comprehensive and in general more 
    conservative than the snubber testing requirements currently contained 
    in TS 15.4.13.
        These changes do not involve a significant increase in the 
    consequences of an accident or event previously evaluated because the 
    source term, containment isolation or radiological releases are not 
    being changed by these proposed revisions. The snubber program ensures 
    that snubbers function as required, therefore related systems continue 
    to function as designed and analyzed. Existing system and component 
    redundancy and operation is not being changed by these proposed 
    changes. The assumptions used in evaluating the radiological 
    consequences in the PBNP Final Safety Analysis Report are not 
    invalidated. Therefore, these changes do not affect the consequences of 
    previously evaluated accidents.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        These changes do not introduce nor increase the number of failure 
    mechanisms of a new or different type than those previously evaluated 
    since there are no physical changes being made to the facility. As 
    noted above, the snubber testing requirements included in the ASME code 
    in general are more comprehensive than the snubber testing requirements 
    currently contained in TS 15.4.13 and provide the requisite level of 
    assurance of snubber operability. The design and design basis of the 
    facility remain unchanged. The plant safety analyses remain unchanged. 
    Therefore, the possibility of a new or different kind of accident from 
    any accident previously evaluated is not introduced.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not involve a significant reduction in a 
    margin of safety.
        The proposed changes do not involve a significant reduction in the 
    margin of safety because existing component redundancy is not being 
    changed by these proposed changes. There are no changes to the initial 
    conditions contributing to accident severity or consequences, and 
    safety margins established through the design and facility license 
    including the Technical Specifications remain unchanged. Therefore, 
    there are no significant reductions in a margin of safety introduced by 
    [these] proposed amendment[s].
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter.
    
    [[Page 71978]]
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: October 7, 1998 (TSCR 207).
        Description of amendment request: The purpose of the proposed 
    amendments is to incorporate changes to the Technical Specifications 
    (TS) to ensure the 4 kV bus undervoltage input to reactor trip is 
    controlled in accordance with the design and licensing basis for the 
    facility. One additional administrative change is requested which 
    removes the footnote related to the definition of Rated Power in TS 
    15.1.j.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of the Point Beach Nuclear Plant [PBNP] in accordance 
    with the proposed amendments will not create a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The changes proposed ensure the Point Beach Nuclear Plant continues 
    to be operated in accordance with the design and licensing basis for 
    the facility.
        The first change removes a footnote qualifying the definition of 
    Rated Power as applied to PBNP Unit 2. This restriction was eliminated 
    with the replacement of Unit 2 steam generators as approved by 
    Amendments 173 and 177, dated July 1, 1997. The analyses for those 
    amendments were performed based on the minimum flow requirements 
    specified in Technical Specification 15.3.1.G.3. The note should have 
    been deleted from the Technical Specifications at that time. 
    Elimination of this note does not result in a change in the operation 
    of PBNP from that analyzed and approved in Amendments 173 and 177. 
    Therefore, this change is administrative and cannot result in an 
    increase in probability or consequences of an accident previously 
    evaluated.
        The second change modifies the Limiting Condition For Operation 
    [LCO] for the undervoltage reactor trip protection function. This trip 
    function is the primary protective function credited in the complete 
    loss of flow event analysis in the Final Safety Analysis Report (FSAR) 
    Section 14.1.8. As a primary protective function, this trip is required 
    to be single failure proof as stipulated in proposed IEEE 279-1968 
    documented in FSAR Section 7.2. This change ensures that this 
    protective feature is maintained in a condition where single failure 
    considerations are satisfied. When single failure criteria cannot be 
    met, appropriate action is stipulated to shutdown the unit placing it 
    in a condition where the protective function is no longer required. 
    Therefore, this change ensures PBNP is operated in accordance with its 
    design and licensing basis and cannot result in an increase in the 
    probability or consequences of an accident previously evaluated.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The changes proposed by this request remove a footnote qualifying 
    the definition of rated power as it applies to PBNP Unit 2 operation, 
    and modify the LCO related to the undervoltage reactor trip protective 
    function to ensure this function is maintained as required by the PBNP 
    design and licensing basis. These changes are in agreement with 
    approved analyses. These changes do not introduce any new accident 
    initiators or alter the response of the PBNP Units to previously 
    analyzed accidents. Therefore, operation of PBNP in accordance with the 
    proposed changes cannot result in a new or different kind of accident 
    from any accident previously evaluated.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not create a significant reduction in a 
    margin of safety.
        Operation of the PBNP in accordance with the proposed amendments is 
    within the bounds of approved design and licensing basis of the 
    facility. The design and licensing basis establish appropriate margins 
    of safety. Since operation of the PBNP remains within the approved 
    design and licensing basis of the facility, a reduction in a margin of 
    safety cannot result.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: November 18, 1998
        Description of amendment request: The proposed amendment would 
    revise the pressure/temperature (P/T) limits and the low-temperature 
    overpressure protection (LTOP) requirements in the facility technical 
    specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change was reviewed in accordance with the provisions 
    of 10 CFR 50.92 to show no significant hazards exist. The proposed 
    change will not:
        (1) Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        Failure of a reactor vessel is not an accident that has been 
    previously evaluated; design provisions ensure that this is not a 
    credible event. Since the potential consequences of a reactor vessel 
    failure are so severe, industry and governmental agencies have worked 
    together to ensure that failure will not occur. Compliance with 10 CFR 
    50 Appendix G and H ensures that failure of a reactor vessel will not 
    occur. The proposed changes do not impact the capability of the reactor 
    coolant pressure boundary piping (i.e., no change in operating 
    pressure, materials, seismic loading, etc.) and therefore do not 
    increase the potential for the occurrence of a LOCA [loss-off-coolant 
    accident].
        The LTOP setpoint, revised enabling temperature, and revised P/T 
    limits reflected in proposed Figures TS 3.1-1 and TS 3.1-2 ensure that 
    the Appendix G pressure/temperature limits are not exceeded, and 
    therefore, ensure that RCS integrity is maintained. The changes do not 
    modify the reactor coolant system pressure boundary, nor make any 
    physical changes to the facility design, material, construction 
    standards, or setpoints. The reactor coolant system full power 
    operating pressure (2235 psig) is not being changed by this proposed 
    amendment. The LTOP valve setpoint remains at less than or equal to 500 
    psig. The LTOP enabling temperature based on Figure
    
    [[Page 71979]]
    
    TS 3.1-2 is 200 deg.F and is consistent with ASME Code Case N-514 
    guidance of RTNDT + 50 deg.F. The revised enabling 
    temperature is lower than the 355 deg.F value in the current TS. 
    However, the allowable combination of Appendix G pressures and 
    temperatures (refer to the 0 deg.F isothermal cooldown limit) is 
    greater for the revised limit curves. The combination of greater 
    allowable Appendix G pressure and temperature limits and lower enabling 
    temperature produces a larger operating window. A larger operating 
    window reduces the likelihood of inadvertently lifting the LTOP relief 
    valve while maneuvering the plant through the knee of the P-T curve 
    during startup and shutdown. The probability of an LTOP event occurring 
    is independent of the pressure-temperature limits for the RCS [reactor 
    coolant system] pressure boundary and enabling temperature. Therefore, 
    the probability of a[n] LTOP event is not increased.
        The revised heatup and cooldown limit curves and LTOP enabling 
    temperature were developed using test results from unirradiated and/or 
    irradiated specimens that represent the KNPP [Kewaunee Nuclear Power 
    Plant] reactor vessel beltline circumferential weld, closure head 
    flange, and intermediate forging. The circumferential beltline weld and 
    intermediate forging are the most limiting materials in the reactor 
    coolant pressure boundary due to the effects of neutron irradiation 
    which cause the flow properties to increase and the toughness to 
    decrease. 10 CFR 50, Appendix G states that the metal temperature of 
    the closure flange regions must exceed the material unirradiated 
    RTNDT by at least 120 deg.F for normal operation and 
    90 deg.F for hydrostatic pressure tests and leak tests when the 
    pressure exceeds 20 percent of the preservice hydrostatic test 
    pressure. Drop weight and Charpy V-notch testing of IP3571 weld metal 
    and the intermediate forging material has been performed and used for 
    derivation of the revised PTS [pressurized thermal shock] assessment, 
    the proposed Appendix G heatup and cooldown limit curves, and the 
    corresponding LTOP system enabling temperature. The revised limit 
    curves and corresponding LTOP enabling temperature have been developed 
    using accepted engineering practices, methods derived from the ASME 
    Boiler and Pressure Vessel Code, criteria set forth in NRC Regulatory 
    Standard Review Plan 5.3.2, and 10 CFR 50.61. Utilization of the 
    revised heatup and cooldown limit curves and corresponding LTOP 
    enabling temperature ensures adequate fracture toughness for ferritic 
    materials of the pressure-retaining components of the reactor coolant 
    pressure boundary. These limit curves provide adequate margins of 
    safety during any condition of normal operation, including anticipated 
    operational occurrences and system hydrostatic tests, and low 
    temperature overpressure protection (corresponding to isothermal events 
    during low temperature operations (i.e., less than or equal to 
    200 deg.F)) thus ensuring the integrity of the reactor coolant pressure 
    boundary.
        The changes do not adversely affect the integrity of the RCS such 
    that its function in the control of radiological consequences is 
    affected. Radiological off-site exposures from normal operation and 
    operational transients, and faults of moderate frequency do not exceed 
    the guidelines of 10 CFR 100. In addition, the changes do not affect 
    any fission product barrier. The changes do not degrade or prevent the 
    response of the LTOP relief valve or other safety-related systems to 
    previously evaluated accidents. In addition, the changes do not alter 
    any assumption previously made in the radiological consequence 
    evaluations nor affect the mitigation of the radiological consequences 
    of an accident previously evaluated. Therefore, the consequences of an 
    accident previously evaluated will not be increased.
        Thus, operation of KNPP in accordance with the PA does not involve 
    a significant increase in the probability or consequences of any 
    accident previously evaluated.
        (2) Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Since the potential consequences of a reactor vessel failure are so 
    severe, industry and governmental agencies have worked together to 
    ensure that failure will not occur. Compliance with 10 CFR 50 Appendix 
    G and H ensures that failure of a reactor vessel will not occur. The 
    proposed heatup and cooldown limit curves have been constructed by 
    combining the most conservative pressure-temperature limits derived by 
    using material properties of the intermediate forging, closure head 
    flange, and beltline circumferential weld to form a single set of 
    composite curves. With NRC approval to use Code Case N-588, the 
    intermediate forging and closure head flange become the controlling 
    materials for development of the heatup limit curve and the cooldown 
    limit curves at low temperatures. At high temperatures, the 
    circumferential weld continues to be limiting for development of the 
    cooldown limit curves. Use of conservative pressure-temperature limits 
    derived by using material properties of the intermediate forging, 
    closure head flange, and beltline circumferential weld to form a single 
    set of composite curves, does not modify the reactor coolant system 
    pressure boundary, nor make any physical changes to the LTOP setpoint 
    or design. Proposed Figures TS 3.1-1 and TS 3.1-2 were prepared in 
    accordance with regulatory and code requirements and were derived using 
    more conservative material property basis and more limiting 
    requirements of neutron exposure projections thru 33 EFPY [effective 
    full-power years] instead of 20 EFPY.
        The revised LTOP system enabling temperature and the proposed 
    Appendix G pressure temperature limitations were prepared using methods 
    derived from the ASME Boiler and Pressure Vessel Code and the criteria 
    set forth in NRC Regulatory Standard Review Plan 5.3.2. The changes do 
    not cause the initiation of any accident nor create any new credible 
    limiting failure for safety-related systems and components. The changes 
    do not result in any event previously deemed incredible being made 
    credible. As such, it does not create the possibility of an accident 
    different than previously evaluated.
        The changes do not have any adverse effect on the ability of the 
    safety-related systems to perform their intended safety functions. The 
    combination of higher allowable Appendix G pressure and temperature 
    limits and lower enabling temperature produces a larger operating 
    window. The ASME Section XI, Working Group on Operating Plant Criteria 
    (WGOPC) has prepared a technical bases document for Code Case N-514. 
    The technical bases document is contained in Attachment 3 of Reference 
    1. This technical bases document provides justification for enabling 
    the LTOP system at temperatures less than 200 deg.F or at coolant 
    temperatures corresponding to a reactor vessel metal temperature less 
    than RTNDT + 50 deg.F, whichever is greater.
        WGOPC, which has responsibility for Appendix G of Section XI, has 
    considered the burden and safety impact imposed by the LTOP criteria, 
    and has developed Code guidelines for determining the LTOP set-point 
    pressure and the required enabling temperature. These guidelines will 
    relieve some operational restrictions, yet provide adequate margins 
    against failure for the reactor vessel. Further, by relieving the 
    operational restrictions, these guidelines result in a reduced
    
    [[Page 71980]]
    
    potential for activation of pressure relieving devices, thereby 
    improving plant safety. Thus, a slightly larger operating window at 
    KNPP is viewed to reduce the likelihood of inadvertently lifting the 
    LTOP relief valve while maneuvering the plant through the knee of the 
    P-T curve during startup and shutdown. The new LTOP operating window 
    (i.e., less than or equal to 200 deg.F) is within the existing 
    operating band for the residual heat removal system; operating 
    procedures allow the LTOP system to be placed into service at 
    <400 deg.f.="" at="" knpp,="" as="" long="" as="" the="" ltop="" relief="" valve="" is="" operable,="" the="" ltop="" system="" is="" enabled="" anytime="" the="" residual="" heat="" removal="" system="" is="" in="" communication="" with="" the="" reactor="" coolant="" system.="" the="" proposed="" changes="" do="" not="" make="" physical="" changes="" to="" the="" plant="" or="" create="" new="" failure="" modes.="" thus,="" the="" pa="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" (3)="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" the="" proposed="" appendix="" g="" pressure="" temperature="" limitations="" and="" ltop="" enabling="" temperature="" were="" prepared="" using="" methods="" derived="" from="" the="" asme="" boiler="" and="" pressure="" vessel="" code,="" including="" code="" cases="" n-514="" and="" n-588,="" and="" the="" criteria="" set="" forth="" in="" nrc="" regulatory="" standard="" review="" plan="" 5.3.2.="" reference="" 1="" to="" this="" letter="" provides="" information="" to="" support="" nrc="" approval="" to="" use="" code="" case="" n-514="" and="" code="" case="" n-588="" for="" the="" knpp="" pts="" evaluation,="" development="" of="" the="" heatup="" and="" cooldown="" limit="" curves,="" and="" establishment="" of="" the="" ltop="" system="" enabling="" temperature.="" these="" documents="" and="" practices="" along="" with="" the="" calculational="" limitations="" specified="" in="" 10="" cfr="" 50.61="" are="" an="" acceptable="" method="" for="" implementing="" the="" requirements="" of="" 10="" cfr="" 50="" appendices="" g="" and="" h.="" use="" of="" the="" methodology="" set="" forth="" in="" the="" asme="" boiler="" and="" pressure="" vessel="" code,="" nrc="" regulatory="" standard="" review="" plan="" 5.3.2.,="" 10="" cfr="" 50.61,="" and="" 10="" cfr="" 50="" appendices="" g="" and="" h="" ensures="" that="" proper="" limits="" and="" safety="" factors="" are="" maintained.="" thus,="" the="" pa="" does="" not="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" the="" revised="" heatup="" and="" cooldown="" limit="" curves="" and="" ltop="" system="" enabling="" temperature="" were="" prepared="" using="" drop="" weight="" and="" charpy="" v-notch="" data="" for="" the="" beltline="" weld,="" closure="" head="" flange,="" and="" intermediated="" forging="" material="" along="" with="" practices="" described="" herein="" and="" methods="" derived="" from="" the="" asme="" boiler="" and="" pressure="" vessel="" code="" and="" 10="" cfr="" 50.61.="" the="" safety="" factors="" and="" margins="" used="" in="" the="" development="" of="" the="" limit="" curves="" and="" ltop="" system="" enabling="" temperature="" meet="" the="" criteria="" set="" forth="" by="" these="" documents.="" application="" of="" low="" leakage="" core="" designs="" decreases="" the="" rate="" of="" shift="" in="" transition="" temperature="" from="" ductile="" to="" nonductile="" behavior.="" the="" revised="" limit="" curves="" and="" ltop="" enabling="" temperature="" provide="" adequate="" margins="" of="" safety="" during="" any="" condition="" of="" normal="" operation,="" including="" anticipated="" operational="" occurrences="" and="" system="" hydrostatic="" tests,="" and="" low="" temperature="" overpressure="" protection="" (corresponding="" to="" isothermal="" events="" during="" low="" temperature="" operations="" (i.e.,="" less="" than="" or="" equal="" to="" 200="" deg.f)).="" with="" the="" preparation="" of="" the="" revised="" limit="" curves="" in="" accordance="" with="" the="" latest="" criteria="" and="" guidance,="" this="" pa="" ensures="" that="" proper="" limits="" and="" safety="" factors="" are="" maintained.="" thus,="" the="" pa="" does="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" university="" of="" wisconsin,="" cofrin="" library,="" 2420="" nicolet="" drive,="" green="" bay,="" wi="" 54311-7001.="" attorney="" for="" licensee:="" bradley="" d.="" jackson,="" esq.,="" foley="" and="" lardner,="" p.o.="" box="" 1497,="" madison,="" wi="" 53701-1497.="" nrc="" project="" director:="" cynthia="" a.="" carpenter.="" previously="" published="" notices="" of="" consideration="" of="" issuance="" of="" amendments="" to="" facility="" operating="" licenses,="" proposed="" no="" significant="" hazards="" consideration="" determination,="" and="" opportunity="" for="" a="" hearing="" the="" following="" notices="" were="" previously="" published="" as="" separate="" individual="" notices.="" the="" notice="" content="" was="" the="" same="" as="" above.="" they="" were="" published="" as="" individual="" notices="" either="" because="" time="" did="" not="" allow="" the="" commission="" to="" wait="" for="" this="" biweekly="" notice="" or="" because="" the="" action="" involved="" exigent="" circumstances.="" they="" are="" repeated="" here="" because="" the="" biweekly="" notice="" lists="" all="" amendments="" issued="" or="" proposed="" to="" be="" issued="" involving="" no="" significant="" hazards="" consideration.="" for="" details,="" see="" the="" individual="" notice="" in="" the="" federal="" register="" on="" the="" day="" and="" page="" cited.="" this="" notice="" does="" not="" extend="" the="" notice="" period="" of="" the="" original="" notice.="" niagara="" mohawk="" power="" corporation,="" docket="" no.="" 50-220,="" nine="" mile="" point="" nuclear="" station="" unit="" no.="" 1,="" oswego="" county,="" new="" york="" date="" of="" application="" for="" amendment:="" may="" 15,="" 1998,="" as="" supplemented="" september="" 25="" and="" october="" 13,="" 1998.="" brief="" description="" of="" amendment:="" the="" amendment="" would="" revise="" technical="" specification="" 5.5,="" ``storage="" of="" unirradiated="" and="" spent="" fuel''="" to="" reflect="" a="" planned="" modification="" to="" increase="" the="" number="" of="" fuel="" assemblies="" that="" can="" be="" stored="" in="" the="" spent="" fuel="" pool="" from="" 2776="" to="" 4086.="" date="" of="" publication="" of="" individual="" notice="" in="" federal="" register:="" november="" 24,="" 1998="" (63="" fr="" 64973).="" expiration="" date="" of="" individual="" notice:="" december="" 24,="" 1998.="" local="" public="" document="" room="" location:="" reference="" and="" documents="" department,="" penfield="" library,="" state="" university="" of="" new="" york,="" oswego,="" new="" york="" 13126.="" notice="" of="" of="" issuance="" of="" amendments="" to="" facility="" operating="" licenses="" during="" the="" period="" since="" publication="" of="" the="" last="" biweekly="" notice,="" the="" commission="" has="" issued="" the="" following="" amendments.="" the="" commission="" has="" determined="" for="" each="" of="" these="" amendments="" that="" the="" application="" complies="" with="" the="" standards="" and="" requirements="" of="" the="" atomic="" energy="" act="" of="" 1954,="" as="" amended="" (the="" act),="" and="" the="" commission's="" rules="" and="" regulations.="" the="" commission="" has="" made="" appropriate="" findings="" as="" required="" by="" the="" act="" and="" the="" commission's="" rules="" and="" regulations="" in="" 10="" cfr="" chapter="" i,="" which="" are="" set="" forth="" in="" the="" license="" amendment.="" notice="" of="" consideration="" of="" issuance="" of="" amendment="" to="" facility="" operating="" license,="" proposed="" no="" significant="" hazards="" consideration="" determination,="" and="" opportunity="" for="" a="" hearing="" in="" connection="" with="" these="" actions="" was="" published="" in="" the="" federal="" register="" as="" indicated.="" unless="" otherwise="" indicated,="" the="" commission="" has="" determined="" that="" these="" amendments="" satisfy="" the="" criteria="" for="" categorical="" exclusion="" in="" accordance="" with="" 10="" cfr="" 51.22.="" therefore,="" pursuant="" to="" 10="" cfr="" 51.22(b),="" no="" environmental="" impact="" statement="" or="" environmental="" assessment="" need="" be="" prepared="" for="" these="" amendments.="" if="" the="" commission="" has="" prepared="" an="" environmental="" assessment="" under="" the="" special="" circumstances="" provision="" in="" 10="" cfr="" 51.12(b)="" and="" has="" made="" a="" determination="" based="" on="" that="" assessment,="" it="" is="" so="" indicated.="" for="" further="" details="" with="" respect="" to="" the="" action="" see="" (1)="" the="" applications="" for="" amendment,="" (2)="" the="" amendment,="" and="" (3)="" [[page="" 71981]]="" the="" commission's="" related="" letter,="" safety="" evaluation="" and/or="" environmental="" assessment="" as="" indicated.="" all="" of="" these="" items="" are="" available="" for="" public="" inspection="" at="" the="" commission's="" public="" document="" room,="" the="" gelman="" building,="" 2120="" l="" street,="" nw.,="" washington,="" dc,="" and="" at="" the="" local="" public="" document="" rooms="" for="" the="" particular="" facilities="" involved.="" baltimore="" gas="" and="" electric="" company,="" docket="" nos.="" 50-317="" and="" 50-318,="" calvert="" cliffs="" nuclear="" power="" plant,="" unit="" nos.="" 1="" and="" 2,="" calvert="" county,="" maryland="" date="" of="" application="" for="" amendments:="" october="" 16,="" 1998.="" brief="" description="" of="" amendments:="" the="" amendments="" revise="" technical="" specification="" (ts)="" 3.3.1="" ``reactor="" protective="" system="" (rps)="" instrumentation-operating''="" and="" ts="" 3.3.2,="" ``reactor="" protective="" system="" (rps)="" instrumentation-shutdown,''="" to="" clarify="" an="" inconsistency="" between="" the="" ts="" wording="" and="" the="" design="" bases="" as="" described="" in="" the="" ts="" bases="" and="" the="" updated="" final="" safety="" analysis="" report.="" specifically,="" the="" change="" replaces="" the="" operating="" bypass="" input="" process="" variable,="" thermal="" power,="" in="" footnotes="" (a),="" (b),="" and="" (d)="" of="" table="" 3.3.1="" and="" in="" the="" note="" to="" limiting="" condition="" for="" operation="" 3.3.2="" with="" nuclear="" instrument="" power.="" date="" of="" issuance:="" december="" 8,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" within="" 30="" days.="" amendment="" nos.:="" 229="" &="" 204.="" facility="" operating="" license="" nos.="" dpr-53="" and="" dpr-69:="" amendments="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" october="" 27,="" 1998="" (63="" fr="" 57320).="" the="" commission's="" related="" evaluation="" of="" these="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 8,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" calvert="" county="" library,="" prince="" frederick,="" maryland="" 20678.="" boston="" edison="" company,="" docket="" no.="" 50-293,="" pilgrim="" nuclear="" power="" station,="" plymouth="" county,="" massachusetts="" date="" of="" application="" for="" amendment:="" april="" 25,="" 1996,="" as="" supplemented="" on="" september="" 5,="" 1996,="" august="" 8,="" 1997,="" march="" 26,="" july="" 31,="" and="" august="" 24,="" 1998.="" brief="" description="" of="" amendment:="" this="" amendment="" revises="" technical="" specifications="" (tss)="" 3/4.5.f.1,="" ``core="" and="" containment="" cooling="" systems''="" to="" extend="" the="" allowed="" outage="" time="" (aot)="" for="" the="" emergency="" diesels,="" tss="" 3.9.b.1="" and="" 3.9.b.4,="" ``auxiliary="" electrical="" system''="" to="" reduce="" the="" aot="" from="" 7="" days="" to="" 3="" days="" and="" reduce="" the="" aot="" for="" the="" combination="" of="" an="" edg="" and="" startup="" transformer="" or="" shutdown="" transformer="" from="" 72="" hours="" to="" 48="" hours,="" and="" add="" configuration="" risk="" management="" program="" in="" ts="" 5.5,="" ``programs="" and="" manuals''="" of="" section="" 5.0="" ``administrative="" controls''.="" various="" ts="" pages="" were="" re-numbered="" in="" section="" 5.0.="" in="" addition,="" tss="" 3.9,="" ``auxiliary="" electrical="" system,''="" and="" 3.9.a,="" ``auxiliary="" electrical="" equipment,''="" have="" been="" reformatted="" to="" be="" consistent="" with="" ts="" 3.9.b="" approved="" in="" a="" previous="" amendment.="" the="" associated="" bases="" sections="" have="" also="" been="" changed="" to="" reflect="" the="" new="" tss.="" date="" of="" issuance:="" december="" 11,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance,="" to="" be="" implemented="" within="" 30="" days.="" amendment="" no.:="" 179.="" facility="" operating="" license="" no.="" dpr-35:="" amendment="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" september="" 23,="" 1998="" (63="" fr="" 50934).="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 11,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" plymouth="" public="" library,="" 11="" north="" street,="" plymouth,="" massachusetts="" 02360.="" duke="" energy="" corporation,="" docket="" nos.="" 50-269,="" 50-270,="" and="" 50-287,="" oconee="" nuclear="" station,="" units="" 1,="" 2,="" and="" 3,="" oconee="" county,="" south="" carolina="" date="" of="" application="" of="" amendments:="" july="" 15,="" 1997,="" as="" supplemented="" march="" 3,="" april="" 13,="" june="" 16,="" october="" 26,="" and="" november="" 5,="" 1998.="" brief="" description="" of="" amendments:="" the="" amendments="" revised="" the="" technical="" specifications="" to="" add="" new="" requirements="" for="" the="" main="" steamline="" break="" instrumentation="" and="" resolved="" issues="" related="" to="" inspection="" and="" enforcement="" bulletin="" 80-04.="" date="" of="" issuance:="" december="" 7,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" coincident="" with="" implementation="" of="" the="" improved="" technical="" specifications.="" amendment="" nos.:="" 234--unit="" 1;="" 234--unit="" 2;="" 233--unit="" 3.="" facility="" operating="" license="" nos.="" dpr-38,="" dpr-47,="" and="" dpr-55:="" amendments="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" september="" 24,="" 1997="" (62="" fr="" 50001).="" the="" march="" 3,="" april="" 13,="" june="" 16,="" october="" 26,="" and="" november="" 5,="" 1998,="" letters="" provided="" clarifying="" information="" that="" did="" not="" change="" the="" scope="" of="" the="" july="" 15,="" 1997,="" application="" and="" the="" initial="" proposed="" no="" significant="" hazards="" consideration="" determination.="" the="" commission's="" related="" evaluation="" of="" the="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 7,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" oconee="" county="" library,="" 501="" west="" south="" broad="" street,="" walhalla,="" south="" carolina.="" duquesne="" light="" company,="" et="" al.,="" docket="" no.="" 50-412,="" beaver="" valley="" power="" station,="" unit="" 2,="" shippingport,="" pennsylvania="" date="" of="" application="" for="" amendment:="" september="" 24,="" 1998,="" as="" supplemented="" november="" 3,="" 1998.="" brief="" description="" of="" amendment:="" this="" amendment="" revised="" technical="" specification="" 3.1.2.8="" in="" two="" places="" to="" change="" the="" term="" ``contained="" volume''="" to="" usable="" volume.''="" this="" change="" eliminates="" the="" potential="" for="" a="" non-conservative="" interpretation="" of="" the="" specification="" values="" for="" the="" refueling="" water="" storage="" tank="" and="" boric="" acid="" storage="" tank="" and="" thereby="" eliminates="" the="" need="" for="" temporary="" administrative="" controls,="" which="" have="" been="" used="" correctly="" to="" properly="" interpret="" the="" specification="" values="" as="" usable="" volumes.="" date="" of="" issuance:="" december="" 14,="" 1998.="" effective="" date:="" effective="" immediately,="" to="" be="" implemented="" within="" 30="" days.="" amendment="" no:="" 95.="" facility="" operating="" license="" no.="" npf-73.="" amendment="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" november="" 4,="" 1998="" (63="" fr="" 59591).="" the="" november="" 3,="" 1998,="" letter="" did="" not="" change="" the="" initial="" proposed="" no="" significant="" hazards="" consideration="" determination="" or="" expand="" the="" amendment="" request="" beyond="" the="" scope="" of="" the="" initial="" notice.="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 14,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" b.="" f.="" jones="" memorial="" library,="" 663="" franklin="" avenue,="" aliquippa,="" pa="" 15001.="" illinois="" power="" company,="" docket="" no.="" 50-461,="" clinton="" power="" station,="" unit="" 1,="" dewitt="" county,="" illinois="" date="" of="" application="" for="" amendment:="" august="" 17,="" 1998.="" [[page="" 71982]]="" brief="" description="" of="" amendment:="" the="" amendment="" reduces="" the="" load="" at="" which="" diesel="" generators="" are="" tested.="" date="" of="" issuance:="" december="" 14,="" 1998.="" effective="" date:="" december="" 14,="" 1998.="" amendment="" no.:="" 118.="" facility="" operating="" license="" no.="" npf-62:="" the="" amendment="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" october="" 7,="" 1998="" (63="" fr="" 53949).="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 14,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" the="" vespasian="" warner="" public="" library,="" 120="" west="" johnson="" street,="" clinton,="" il="" 61727.="" indiana="" michigan="" power="" company,="" docket="" nos.="" 50-315="" and="" 50-316,="" donald="" c.="" cook="" nuclear="" plant,="" units="" 1="" and="" 2,="" berrien="" county,="" michigan="" date="" of="" application="" for="" amendments:="" august="" 1,="" 1997.="" brief="" description="" of="" amendments:="" the="" amendments="" delete="" a="" portion="" of="" a="" technical="" specifications="" surveillance="" test="" requirement="" that="" specifies="" that="" the="" steam="" driven="" auxiliary="" feedwater="" pumps="" be="" tested="" ``when="" the="" secondary="" steam="" supply="" pressure="" is="" greater="" than="" 310="" psig.''="" this="" removes="" any="" misunderstanding="" that="" the="" secondary="" steam="" pressure="" must="" be="" just="" above="" 310="" psig="" for="" this="" test.="" date="" of="" issuance:="" december="" 10,="" 1998.="" effective="" date:="" december="" 10,="" 1998,="" with="" full="" implementation="" within="" 45="" days.="" amendment="" nos.:="" 225="" and="" 209.="" facility="" operating="" license="" nos.="" dpr-58="" and="" dpr-74:="" amendments="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" december="" 31,="" 1997="" (62="" fr="" 68308).="" the="" commission's="" related="" evaluation="" of="" the="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 10,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" maud="" preston="" palenske="" memorial="" library,="" 500="" market="" street,="" st.="" joseph,="" mi="" 49085.="" niagara="" mohawk="" power="" corporation,="" docket="" no.="" 50-410,="" nine="" mile="" point="" nuclear="" station="" unit="" no.="" 2,="" oswego="" county,="" new="" york="" date="" of="" application="" for="" amendment:="" february="" 5,="" 1998.="" brief="" description="" of="" amendment:="" this="" amendment="" changes="" the="" technical="" specifications="" to="" update="" the="" terminology="" and="" references="" to="" 10="" cfr="" 50.55a(f)="" and="" (g)="" consistent="" with="" the="" 1989="" edition="" of="" section="" xi="" of="" the="" american="" society="" of="" mechanical="" engineers="" boiler="" and="" pressure="" vessel="" code,="" and="" consistent="" with="" the="" second="" 10-year="" interval="" of="" the="" inservice="" inspections="" and="" inservice="" testing="" program="" plans.="" date="" of="" issuance:="" december="" 3,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" within="" 30="" days.="" amendment="" no.:="" 84="" facility="" operating="" license="" no.="" dpr-63:="" amendment="" revises="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" march="" 11,="" 1998="" (63="" fr="" 11920).="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 3,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" reference="" and="" documents="" department,="" penfield="" library,="" state="" university="" of="" new="" york,="" oswego,="" new="" york="" 13126.="" peco="" energy="" company,="" docket="" nos.="" 50-352="" and="" 50-353,="" limerick="" generating="" station,="" units="" 1="" and="" 2,="" montgomery="" county,="" pennsylvania="" date="" of="" application="" for="" amendments:="" august="" 8,="" 1996,="" as="" supplemented="" june="" 30,="" 1997="" and="" august="" 26,="" 1998.="" brief="" description="" of="" amendments:="" the="" amendments="" eliminate="" the="" response="" time="" testing="" requirements="" for="" selected="" sensors="" and="" specified="" instrument="" loops="" for="" (1)="" the="" reactor="" protection="" system,="" (2)="" the="" isolation="" system,="" and="" (3)="" the="" emergency="" core="" cooling="" system.="" date="" of="" issuance:="" december="" 14,="" 1998.="" effective="" date:="" both="" units,="" as="" of="" date="" of="" issuance,="" to="" be="" implemented="" within="" 30="" days.="" amendment="" nos.:="" 132="" and="" 93.="" facility="" operating="" license="" nos.="" npf-39="" and="" npf-85:="" the="" amendments="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" november="" 6,="" 1996="" (61="" fr="" 57489).="" the="" june="" 30,="" 1997="" and="" august="" 26,="" 1998,="" letters="" provided="" clarifying="" information="" that="" did="" not="" change="" the="" initial="" proposed="" no="" significant="" hazards="" consideration="" determination.="" the="" commission's="" related="" evaluation="" of="" the="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 14,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" pottstown="" public="" library,="" 500="" high="" street,="" pottstown,="" pa="" 19464.="" power="" authority="" of="" the="" state="" of="" new="" york,="" docket="" no.="" 50-333,="" james="" a.="" fitzpatrick="" nuclear="" power="" plant,="" oswego="" county,="" new="" york="" date="" of="" application="" for="" amendment:="" july="" 10,="" 1998,="" as="" supplemented="" october="" 16,="" 1998.="" brief="" description="" of="" amendment:="" the="" amendment="" revised="" technical="" specification="" (ts)="" 3.6/4.6="" and="" associated="" bases="" to="" relocate="" portions="" of="" the="" reactor="" coolant="" chemistry="" to="" the="" updated="" final="" safety="" analysis="" report="" and="" to="" applicable="" plant="" procedures.="" changes="" to="" the="" relocated="" requirements="" will="" be="" controlled="" by="" the="" provisions="" of="" 10="" cfr="" 50.59.="" date="" of="" issuance:="" december="" 1,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" within="" 30="" days.="" amendment="" no.:="" 247.="" facility="" operating="" license="" no.="" dpr-59:="" amendment="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" july="" 29,="" 1998="" (63="" fr="" 40560).="" the="" october="" 16,="" 1998,="" submittal="" fell="" with="" the="" scope="" of,="" and="" did="" not="" change,="" the="" initial="" proposed="" finding="" of="" no="" significant="" hazards="" consideration.="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 1,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" reference="" and="" documents="" department,="" penfield="" library,="" state="" university="" of="" new="" york,="" oswego,="" new="" york="" 13126.="" power="" authority="" of="" the="" state="" of="" new="" york,="" docket="" no.="" 50-333,="" james="" a.="" fitzpatrick="" nuclear="" power="" plant,="" oswego="" county,="" new="" york="" date="" of="" application="" for="" amendment:="" march="" 30,="" 1998,="" as="" supplemented="" on="" october="" 27,="" 1998.="" brief="" description="" of="" amendment:="" the="" amendment="" revises="" the="" definition="" of="" logic="" system="" functional="" tests,="" and="" revises="" test="" frequency="" requirements="" for="" certain="" instrumentation.="" date="" of="" issuance:="" december="" 11,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" within="" 30="" days.="" amendment="" no.:="" 248.="" facility="" operating="" license="" no.="" dpr-59:="" amendment="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" april="" 22,="" 1998="" (63="" fr="" 19978).="" the="" october="" 27,="" 1998,="" supplemental="" letter="" provided="" clarifying="" information="" that="" did="" not="" change="" the="" initial="" proposed="" no="" significant="" hazards="" consideration.="" [[page="" 71983]]="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 11,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" reference="" and="" documents="" department,="" penfield="" library,="" state="" university="" of="" new="" york,="" oswego,="" new="" york="" 13126="" public="" service="" electric="" &="" gas="" company,="" docket="" nos.="" 50-272="" and="" 50-311,="" salem="" nuclear="" generating="" station,="" unit="" nos.="" 1="" and="" 2,="" salem="" county,="" new="" jersey="" date="" of="" application="" for="" amendments:="" august="" 12,="" 1998,="" as="" supplemented="" on="" october="" 12,="" 1998.="" the="" october="" 12,="" 1998,="" letter="" provided="" clarifying="" information="" that="" did="" not="" change="" the="" initial="" proposed="" no="" sigificant="" hazards="" consideration="" determination.="" brief="" description="" of="" amendments:="" the="" amendments="" revise="" ts="" 3/="" 4.6.1.3,="" ``containment="" air="" locks,''="" to="" change="" the="" action="" statements="" for="" an="" inoperable="" air="" lock.="" the="" amendments="" also="" revise="" ts="" bases="" 3/4.6.1.2,="" ``containment="" leakage,''="" to="" correct="" an="" editorial="" error="" and="" ts="" bases="" 3/="" 4.6.1.3,="" ``containment="" air="" locks,''="" to="" provide="" additional="" details="" regarding="" the="" air="" locks.="" date="" of="" issuance:="" december="" 2,="" 1998.="" effective="" date:="" december="" 2,="" 1998.="" amendment="" nos:="" 215="" and="" 195.="" facility="" operating="" license="" nos.="" dpr-70="" and="" dpr-75:="" the="" amendments="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" september="" 9,="" 1998="" (63="" fr="" 48265).="" the="" commission's="" related="" evaluation="" of="" the="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 2,="" 1998="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" salem="" free="" public="" library,="" 112="" west="" broadway,="" salem,="" nj="" 08079.="" southern="" nuclear="" operating="" company,="" inc.,="" docket="" nos.="" 50-348="" and="" 50-="" 364,="" joseph="" m.="" farley="" nuclear="" plant,="" units="" 1="" and="" 2,="" houston="" county,="" alabama="" date="" of="" amendments="" request:="" december="" 31,="" 1997,="" as="" supplemented="" by="" letter="" dated="" september="" 11,="" 1998.="" brief="" description="" of="" amendments:="" the="" amendments="" revised="" the="" technical="" specifications="" (tss)="" to="" change="" the="" intermediate="" range="" neutron="" flux="" reactor="" trip="" setpoint="" and="" allowable="" value,="" and="" delete="" the="" reference="" to="" the="" reactor="" trip="" setpoints="" in="" ts="" 3.10.3,="" ``special="" test="" exceptions--physics="" tests,''="" and="" ts="" 3.10.4,="" ``special="" test="" exceptions--="" reactor="" coolant="" loops.''="" date="" of="" issuance:="" december="" 8,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" within="" 30="" days="" from="" the="" date="" of="" issuance.="" amendment="" nos.:="" unit="" 1--140;="" unit="" 2--132.="" facility="" operating="" license="" nos.="" npf-2="" and="" npf-8:="" amendments="" revise="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" february="" 11,="" 1998="" (63="" fr="" 6998).="" the="" september="" 11,="" 1998,="" letter="" provided="" clarifying="" information="" that="" did="" not="" change="" december="" 31,="" 1997,="" application="" or="" the="" initial="" proposed="" no="" significant="" hazards="" consideration="" determination.="" the="" commission's="" related="" evaluation="" of="" the="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 8,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" houston-love="" memorial="" library,="" 212="" w.="" burdeshaw="" street,="" post="" office="" box="" 1369,="" dothan,="" alabama.="" tennessee="" valley="" authority,="" docket="" nos.="" 50-327="" and="" 50-328,="" sequoyah="" nuclear="" plant,="" units="" 1="" and="" 2,="" hamilton="" county,="" tennessee="" date="" of="" application="" for="" amendments:="" september="" 20,="" 1996="" (ts="" 96-09).="" brief="" description="" of="" amendments:="" the="" amendments="" change="" the="" technical="" specifications="" to="" clarify="" the="" types="" of="" work="" shifts="" that="" are="" acceptable="" when="" considering="" the="" requirements="" to="" ensure="" overtime="" is="" not="" heavily="" used="" on="" a="" routine="" basis="" by="" unit="" staff.="" date="" of="" issuance:="" december="" 7,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" no="" later="" than="" 45="" days="" after="" issuance.="" amendment="" nos.:="" 240="" and="" 230.="" facility="" operating="" license="" nos.="" dpr-77="" and="" dpr-79:="" amendments="" revise="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" november="" 4,="" 1998="" (63="" fr="" 59596).="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 7,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" chattanooga-hamilton="" county="" library,="" 1001="" broad="" street,="" chattanooga,="" tennessee="" 37402.="" tennessee="" valley="" authority,="" docket="" nos.="" 50-327="" and="" 50-328,="" sequoyah="" nuclear="" plant,="" units="" 1="" and="" 2,="" hamilton="" county,="" tennessee="" date="" of="" application="" for="" amendments:="" august="" 22,="" 1998,="" as="" supplemented="" on="" august="" 27="" and="" october="" 8,="" 1998="" (ts="" 96-08).="" the="" august="" 27,="" 1998,="" amendment="" request="" superseded="" the="" original="" (august="" 22,="" 1998)="" request="" in="" its="" entirety.="" brief="" description="" of="" amendments:="" the="" amendments="" revise="" the="" sequoyah="" nuclear="" plant="" technical="" specifications="" by="" extending="" the="" allowed="" outage="" time="" for="" the="" sqn="" emergency="" diesel="" generators="" from="" 72="" hours="" to="" 7="" days.="" date="" of="" issuance:="" december="" 16,="" 1998.="" effective="" date:="" as="" of="" the="" date="" of="" issuance="" to="" be="" implemented="" no="" later="" than="" 45="" days="" after="" issuance.="" amendment="" nos.:="" 241="" and="" 231.="" facility="" operating="" license="" nos.="" dpr-77="" and="" dpr-79:="" amendments="" revise="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" october="" 9,="" 1996="" (61="" fr="" 52969),="" superseded="" by="" a="" second="" notice="" on="" september="" 9,="" 1998="" (63="" fr="" 48270).="" the="" october="" 8,="" 1998,="" letter="" provided="" clarifying="" information="" that="" did="" not="" change="" the="" initial="" no="" significant="" hazards="" consideration="" determination.="" the="" commission's="" related="" evaluation="" of="" the="" amendment="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 16,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" chattanooga-hamilton="" county="" library,="" 1001="" broad="" street,="" chattanooga,="" tennessee="" 37402.="" virginia="" electric="" and="" power="" company,="" et="" al.,="" docket="" nos.="" 50-338="" and="" 50-="" 339,="" north="" anna="" power="" station,="" units="" no.="" 1="" and="" no.="" 2,="" louisa="" county,="" virginia="" date="" of="" application="" for="" amendments:="" july="" 28,="" 1998,="" as="" supplemented="" october="" 16,="" 1998.="" the="" october="" 16,="" 1998,="" letter="" was="" administrative="" in="" nature="" and="" did="" not="" change="" the="" initial="" no="" significant="" hazards="" consideration="" determination.="" brief="" description="" of="" amendments:="" the="" amendments="" revise="" the="" technical="" specifications="" to="" change="" the="" emergency="" diesel="" generator="" section="" to="" be="" consistent="" with="" station="" procedures="" associated="" with="" steady-state="" conditions.="" date="" of="" issuance:="" december="" 10,="" 1998.="" effective="" date:="" december="" 10,="" 1998.="" amendment="" nos.:="" 216="" and="" 197.="" facility="" operating="" license="" nos.="" npf-4="" and="" npf-7:="" amendments="" revised="" the="" technical="" specifications.="" date="" of="" initial="" notice="" in="" federal="" register:="" september="" 9,="" 1998="" (63="" fr="" 48272).="" the="" commission's="" related="" evaluation="" of="" the="" amendments="" is="" contained="" in="" a="" safety="" evaluation="" dated="" december="" 10,="" 1998.="" no="" significant="" hazards="" consideration="" comments="" received:="" no.="" local="" public="" document="" room="" location:="" the="" alderman="" library,="" special="" [[page="" 71984]]="" collections="" department,="" university="" of="" virginia,="" charlottesville,="" virginia="" 22903-2498.="" dated="" at="" rockville,="" maryland,="" this="" 23rd="" day="" of="" december="" 1998.="" for="" the="" nuclear="" regulatory="" commission.="" elinor="" g.="" adensam,="" acting="" director,="" division="" of="" reactor="" projects--iii/iv,="" office="" of="" nuclear="" reactor="" regulation.="" [fr="" doc.="" 98-34440="" filed="" 12-29-98;="" 8:45="" am]="" billing="" code="" 7590-01-p="">

Document Information

Published:
12/30/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-34440
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
71962-71984 (23 pages)
PDF File:
98-34440.pdf