97-33968. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 250 (Wednesday, December 31, 1997)]
    [Notices]
    [Pages 68303-68323]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-33968]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Pub. L. 97-415, the U.S. Nuclear Regulatory Commission 
    (the Commission or NRC staff) is publishing this regular biweekly 
    notice. Pub. L. 97-415 revised section 189 of the Atomic Energy Act of 
    1954, as amended (the Act), to require the Commission to publish notice 
    of any amendments issued, or proposed to be issued, under a new 
    provision of section 189 of the Act. This provision grants the 
    Commission the authority to issue and make immediately effective any 
    amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from December 6, 1997, through December 18, 1997. 
    The last biweekly notice was published on December 17, 1997 (62 FR 
    66133).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and should cite the publication date and 
    page number of this Federal Register notice. Written comments may also 
    be delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By January 30, 1998, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board
    
    [[Page 68304]]
    
    Panel, will rule on the request and/or petition; and the Secretary or 
    the designated Atomic Safety and Licensing Board will issue a notice of 
    a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al.
    
    [Docket Nos. 50-325 and 50-324]
    
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of amendments request: November 26, 1997.
        Description of amendments request: Carolina Power & Light Company 
    (CP&L) has proposed amendments to the Technical Specifications (TS) for 
    the Brunswick Steam Electric Plant Units 1 and 2 (BSEP 1 & 2) to revise 
    certain instrumentation allowable values. The revised values were 
    calculated using a methodology and format consistent with that provided 
    in NUREG-1433, Revision 1, ``Standard Technical Specifications General 
    Electric Plants, BWR/4.'' The current TS are based on the uncertainty 
    associated with the trip unit portion of the instrumentation circuitry. 
    The proposed values are based on the uncertainty associated with the 
    entire instrumentation loop (sensor and trip unit). The NRC has 
    previously approved this methodology for BSEP 1 & 2 as part of a 5 
    percent power uprate amendment dated November 1, 1996.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendments do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes affect accident mitigation instrumentation 
    allowable values. The changes will not affect the accident 
    mitigation instrumentation functions. No changes will occur in the 
    way in which equipment is operated. Therefore, the probability of a 
    previously evaluated accident can not be affected.
        The proposed changes establish the allowable values for certain 
    functions in accordance with the CP&L setpoint methodology, which 
    has been approved, by the NRC, for use at the BSEP. The proposed 
    changes do not affect the actual instrument setpoints. The proposed 
    allowable values were calculated by applying calibration based 
    errors to the trip setpoint values; thereby establishing an 
    operability limit associated with the entire loop of an 
    instrumentation function to ensure sufficient margin to protect 
    analytical limits. The changes do not affect the analytical limits 
    associated with the involved instrumentation functions. The involved 
    instrumentation will continue to perform its accident mitigation 
    functions as designed. Therefore, the consequences of a previously 
    evaluated accident are not increased.
        2. The proposed amendments would not create the possibility of a 
    new or different
    
    [[Page 68305]]
    
    kind of accident from any accident previously evaluated.
        The proposed changes do not affect the actual instrument 
    setpoints nor do they affect the accident mitigation instrumentation 
    functions. No changes will occur in the way in which equipment is 
    operated. The involved instrumentation will continue to perform its 
    accident mitigation functions as designed. Therefore, the proposed 
    license amendments can not create the possibility of a new or 
    different kind of accident.
        3. The proposed license amendments do not involve a significant 
    reduction in a margin of safety.
        The proposed changes affect accident mitigation instrumentation 
    allowable values. The changes will not affect the accident 
    mitigation instrumentation functions. No changes will occur in the 
    way in which equipment is operated. The proposed changes establish 
    the allowable values for certain functions in accordance with the 
    CP&L setpoint methodology which has been approved, by the NRC, for 
    use at the BSEP. The proposed allowable values were calculated by 
    applying calibration based errors to the trip setpoint values; 
    thereby establishing an operability limit associated with the entire 
    loop of an instrumentation function to ensure sufficient margin to 
    protect analytical limits. The changes do not affect the analytical 
    limits associated with the involved instrumentation functions. The 
    involved instrumentation will continue to perform its accident 
    mitigation functions as designed. Therefore, the proposed license 
    amendments do not involve a significant reduction in the margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: James E. Lyons.
    
    Carolina Power & Light Company, et al.
    
    Docket No. 50-400, Shearon Harris
    
    Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North Carolina
    
        Date of amendment request: October 29, 1997.
        Description of amendment request: Technical Specifications (TS) 
    3.8.1.1.a.3, 3.8.1.1.b.4, and 3.8.1.1.d.2 presently require a plant 
    shutdown and declaring the redundant required feature inoperable, when 
    the required feature powered from the operable A.C. source is 
    inoperable. The proposed change clarifies the intent of this TS to 
    permit the applicable redundant required feature TS to direct a plant 
    shutdown when required. The proposed amendment changes the existing TS 
    3.8.1.1.a.3, 3.8.1.1.b.4, and 3.8.1.1.d.2 to eliminate the separate 
    requirement for plant shutdown and instead allows the applicable 
    required redundant feature TS to direct the plant shutdown when 
    required.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        This change does not involve a significant hazards consideration 
    for the following reasons:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment will not introduce any new equipment or 
    require existing equipment to function different from that 
    previously evaluated in the Final Safety Analysis Report (FSAR) or 
    TS. The changes are consistent with NUREG-1431 and the Commission's 
    Final Policy Statement on Technical Specification improvements.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment will not introduce any new equipment or 
    require existing equipment to function different from that 
    previously evaluated in the Final Safety Analysis Report (FSAR) or 
    TS. The changes are consistent with NUREG-1431 and the Commission's 
    Final Policy Statement on Technical Specification improvements. The 
    proposed amendment will not create any new accident scenarios, 
    because the change does not introduce any new single failures, 
    adverse equipment or material interactions, or release paths.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        Margin of safety for acceptable TS action times have been 
    determined for each TS related system. The proposed change will not 
    alter individual system TS action times. HNP [the Harris Nuclear 
    Plant] proposes to change the requirement to shutdown after 
    expiration of the completion time of an inoperable A.C. source 
    concurrent with an inoperable required feature. Instead of requiring 
    a shutdown, the required feature on the inoperable A.C. source will 
    be declared inoperable and the individual TS will be implemented.
        In most cases with both redundant features inoperable, a plant 
    shutdown will be required by TS 3.0.3. In the few instances where 
    additional time is allowed by the individual TS for both redundant 
    required features being inoperable, then an immediate plant shutdown 
    would not be required. The allowed out of service time for loss of 
    individual safety functions has been previously analyzed for HNP TS 
    and NUREG-1431, Revision 1.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: James E. Lyons.
    
    Florida Power and Light Company, et al.
    
    [Docket Nos. 50-335 and 50-389]
    
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: December 1, 1997.
        Description of amendment request: The proposed amendment revises 
    the Unit 1 and Unit 2 Environmental Protection Plans (EPP) Section 4, 
    ``Environmental Conditions,'' and Section 5, ``Administrative 
    Procedures,'' to incorporate the proposed terms and conditions of the 
    Incidental Take Statement included in the Biological Opinion issued by 
    the National Marine Fisheries Service (NMFS) on February 7, 1997. The 
    proposed amendment also revises the wording in the Unit 1 EPP to make 
    it consistent with the Unit 2 EPP.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the
    
    [[Page 68306]]
    
    probability or consequences of an accident previously evaluated.
        The changes are administrative in nature and would in no way 
    affect the initial conditions, assumptions, or conclusions of the 
    St. Lucie Unit 1 or Unit 2, accident analyses. In addition, the 
    proposed changes would not affect the operation or performance of 
    any equipment assumed in the accident analyses.
        Based on the above information, we conclude that the proposed 
    changes would not significantly increase the probability or 
    consequences of an accident previously evaluated.
        (2) Use of the modified specification would not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The changes are administrative in nature and would in no way 
    impact or alter the configuration or operation of the facilities and 
    would create no new modes of operation. We conclude that the 
    proposed changes would not create the possibility of a new or 
    different kind of accident.
        (3) Use of the modified specification would not involve a 
    significant reduction in a margin of safety.
        As indicated in the discussion of Criterion 1, the changes are 
    administrative in nature and would in no way affect plant or 
    equipment operation or the accident analysis. We conclude that the 
    proposed changes would not result in a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Community College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34981-5596.
        Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420.
        NRC Project Director: Frederick J. Hebdon.
    
    IES Utilities Inc.
    
    [Docket No. 50-331]
    
    Duane Arnold Energy Center, Linn County, Iowa
    
        Date of amendment request: October 30, 1996.
        Description of amendment request: The proposed amendment, included 
    as part of the proposed conversion from current Technical 
    Specifications (CTS) to improved Technical Specifications (ITS), would 
    modify the Surveillance Requirements (SRs) recommended in NUREG-1433 
    LOC 3.5.1 by revising the combinations (Conditions C, D, G, and I of 
    ITS 3.5.1) of emergency core cooling systems/subsystems that may be out 
    of service. The combinations are supported by the Duane Arnold Energy 
    Center (DAEC) Loss-of-Coolant Accident (LOCA) analysis.
    Condition C
        ITS 3.5.1  Action C establishes Required Actions and Completion 
    Times for the situation when one core spray (CS) subsystem and one or 
    two residual heat removal (RHR) pump(s) are inoperable. The proposed 
    specification is less restrictive than CTS 3.5.A.4, which allows one 
    RHR pump to be inoperable for 30 days, and CTS 3.5.A.5, which allows 
    two RHR pumps (i.e., the low pressure coolant injection (LPCI) 
    subsystem) to be inoperable for up to 7 days, provided the remaining 
    RHR (i.e., LPCI) active components, both CS subsystems, the containment 
    spray subsystem, and the diesel generators are verified to be operable. 
    The CTS does not allow one CS subsystem and one or two RHR pump(s) to 
    be inoperable at the same time. The LOCA analysis presented in NEDC-
    31310P, (Duane Arnold Energy Center SAFER/GESTR-LOCA Loss-of-Coolant 
    Accident Analysis), indicates that an adequate level of protection is 
    provided by the remaining operable ECCS subsystems. The accident 
    analysis also demonstrates that in this condition, the peak clad 
    temperature remains below the regulatory limit. However, another single 
    failure may place the plant in a condition where adequate core cooling 
    may not be available during a DBA-LOCA. Therefore, a Completion Time of 
    72 hours has been proposed to either restore the inoperable CS 
    subsystem or the inoperable RHR pump(s).
    Condition D
        ITS 3.5.1  Action D establishes Required Actions and Completion 
    Times for the situation when two CS subsystems are inoperable. The 
    proposed specification is less restrictive than CTS 3.5.A.2, which 
    allows only one CS subsystem to be inoperable. CTS 3.5.A.6 would 
    require the plant to be in Hot Shutdown within 12 hours and Cold 
    Shutdown within the following 24 hours if both CS subsystems were 
    inoperable. With two CS subsystems inoperable, the LOCA analysis 
    presented in NEDC-31310P, (Duane Arnold Energy Center SAFER/GESTR-LOCA 
    Loss-of-Coolant Accident Analysis), indicates that the remaining 
    operable low pressure ECCS subsystem consisting of LPCI with four RHR 
    pumps operable (only 3 pumps required), provides adequate protection. 
    However, another single failure may place the plant in a condition 
    where adequate core cooling may not be available during a Design Basis 
    Accident LOCA. Therefore, a Completion Time of 72 hours has been 
    proposed to restore one CS subsystem to operable status.
    Condition G
        ITS 3.5.1 Action G establishes Required Actions and Completion 
    Times for the situation when HPCI and one RHR pump are inoperable. The 
    proposed specification is less restrictive than CTS 3.5.D.2, which 
    allows continued operation if HPCI is inoperable only if both CSs, 
    LPCI, ADS, and RCIC are verified to be operable. While the LPCI 
    subsystem is technically operable with only 3 of 4 RHR pumps operable, 
    the CTS is currently interpreted by DAEC to require all 4 RHR pumps to 
    be operable for the requirements of CTS 3.5.D.2 to be met, as a single 
    RHR pump has more makeup capability than the HPCI System. Thus for 
    mitigating small and intermediate break LOCAs, one LPCI pump, in 
    combination with ADS, is more than adequate core cooling. The condition 
    of when HPCI and one RHR pump are inoperable is bounded by the analysis 
    in NEDC-31310P, Duane Arnold Energy Center, SAFER/GESTR-LOCA Loss-of-
    Coolant Accident Analysis. Since the remaining operable low pressure 
    ECCS subsystems are more than capable of performing their intended 
    function, and RCIC and ADS are Operable, the proposed Action G 
    maintains LOCA analysis assumptions for ECCS Operability. The proposed 
    ITS condition allows 7 days to restore the HPCI System or the RHR pump 
    to operable status. The licensee considers the 7 day Completion Time 
    reasonable in that the LOCA analysis demonstrates that in this 
    condition, the peak clad temperature remains below the regulatory 
    limit. The 7 day Completion Time also provides the benefit of 
    potentially avoiding an unnecessary plant shutdown while the safety 
    functions are still capable of being performed.
    Condition I
        ITS 3.5.1 Action I establishes Required Actions and Completion 
    Times for the situation when HPCI and one ADS valve are inoperable. The 
    proposed Specification is less restrictive than CTS 3.5.D.2, which 
    allows continued operation if HPCI is inoperable only if both CSs, 
    LPCI, ADS, and RCIC are verified to be operable. While ADS is capable 
    of performing its design function with only 3 of 4 valves operable, per 
    NEDC-31310P, Duane Arnold Energy Center, SAFER/GESTR-
    
    [[Page 68307]]
    
    LOCA Loss-of-Coolant Accident Analysis, the CTS requires all 4 ADS 
    valves to be operable for the requirements of CTS 3.5.D.2 to be met. 
    The proposed specification is less restrictive than CTS 3.5.F.2, which 
    allows continued operation when one ADS valve is inoperable only if 
    HPCI is verified to be operable. Since all low pressure ECCS subsystems 
    remain capable of performing their design function and ADS is still 
    capable of performing its design function, ITS 3.5.1 Action I maintains 
    LOCA assumptions to ensure an adequate level of protection is 
    maintained. The proposed condition allows 72 hours to restore the HPCI 
    system or the ADS valve to operable status, since another single 
    failure (i.e., loss of another ADS valve), may place the plant in a 
    condition where adequate core cooling may not be available during a 
    small or intermediate break LOCA.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    For Condition C
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change will allow one Core Spray subsystem and one 
    or two RHR pump(s) to be inoperable for up to 72 hours. The ECCS 
    subsystems affected by this change are not assumed to be initiators 
    of analyzed events. Therefore, the proposed change does not increase 
    the probability of any accident. The role of these ECCS subsystems 
    is in the mitigation of accident consequences. The proposed change 
    does not allow unlimited continuous operation with the plant in a 
    condition where an additional single failure could result in a loss 
    of ECCS function. The proposed change does not increase the 
    consequences of an accident because accident analysis presented in 
    NEDC-31310P, Duane Arnold Energy Center SAFER/GESTR-LOCA Loss-of-
    Coolant Accident Analysis, indicates that an adequate level of 
    protection is maintained by the ADS System and the remaining 
    Operable ECCS subsystems when one Core Spray subsystem and one or 
    two RHR pump(s) are inoperable. Therefore, this change will not 
    involve a significant increase in the consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change will not involve any physical changes to 
    plant systems, structures, or components (SSCs), or the manner in 
    which these SSCs are operated, maintained, modified, tested or 
    inspected. The change ensures the remaining ECCS capability is 
    adequate to mitigate the consequences of accidents. Therefore, this 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change does not significantly reduce the margin of 
    safety because accident analysis presented in NEDC-31310P, Duane 
    Arnold Energy Center SAFER/GESTR-LOCA Loss-of-Coolant Accident 
    Analysis, indicates that the plant is protected by the ADS System 
    and the remaining ECCS subsystems when one Core Spray subsystem and 
    one or two RHR pump(s) are inoperable. The accident analysis 
    demonstrates that in this condition, the peak clad temperature 
    remains below the regulatory limit. However, with one Core Spray 
    subsystem and one or two RHR pump(s) inoperable, another single 
    failure may place the plant in a condition where adequate core 
    cooling may not be available during a DBA-LOCA. Therefore, a 
    Completion Time of 72 hours has been assigned to either restore the 
    inoperable Core Spray subsystem or the RHR pump. In addition, this 
    change provides the benefit of potentially avoiding an unnecessary 
    plant shutdown (due to a Completion Time being provided for one Core 
    Spray subsystem and one or two RHR pump(s)) when the remaining ECCS 
    subsystems and the ADS are capable of mitigating potential events. 
    Therefore, this change does not involve a significant reduction in a 
    martin safety.
    
    For Condition D
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change will allow both Core Spray subsystems to be 
    inoperable for up to 72 hours. The ECCS subsystems affected by this 
    change are not assumed to be initiators of analyzed events. 
    Therefore, the proposed change does not increase the probability of 
    any accident. The role of these ECCS subsystems is in the mitigation 
    of accident consequences. The proposed change does not allow 
    unlimited continuous operation with the plant in a condition where 
    an additional single failure could result in a loss of ECCS 
    function. The proposed change does not increase the consequences of 
    an accident because accident analysis presented in NEDC-3131OP, 
    Duane Arnold Energy Center SAFER/GESTR-LOCA Loss-of-Coolant Accident 
    Analysis, indicates that an adequate level of protection is 
    maintained by the ADS System and remaining Operable ECCS subsystem 
    when two Core Spray subsystems or inoperable. Therefore, this change 
    will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change will not involve any physical changes to 
    plant systems, structures, or components (SSCs), or the manner in 
    which these SSCs are operated, maintained, modified, tested, or 
    inspected. The change ensures the remaining ECCS capability is 
    adequate to mitigate the consequences of accidents. Therefore, this 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change does not significantly reduce the margin of 
    safety because accident analysis presented in NEDC-31310P, Duane 
    Arnold Energy Center SAFER/GESTR-LOCA Loss-of-Coolant Accident 
    Analysis, indicates that the plant is protected by the ADS System 
    and the remaining ECCS subsystem when two Core Spray subsystems are 
    inoperable. The accident analysis demonstrates that in this 
    condition, the peak clad temperature remains below the regulatory 
    limit. However, with both Core Spray subsystems inoperable, another 
    single failure may place the plant in a condition where adequate 
    core cooling may not be available during a DBA-LOCA. Therefore, a 
    Completion Time of 72 hours has been assigned to restore one 
    inoperable Core Spray subsystem. In addition this change provides 
    the benefit of potentially avoiding an unnecessary plant shutdown 
    (due to a Completion Time being provided for both Core Spray 
    subsystems inoperable) when the remaining ECCS subsystem and the ADS 
    are capable of mitigating potential events. Therefore, this change 
    does not involve a significant reduction in a margin of safety.
    
    Condition G
    
        1. Does the change involve a significant increase in the 
    probability or consequences or an accident previously evaluated?
        The proposed change will allow the HPCI System and one RHR pump 
    to be inoperable for up to 7 days. The ECCS subsystems affected by 
    this change are not assumed to be initiators of analyzed events. 
    Therefore, the proposed change does not increase the probability of 
    any accident. The role of these ECCS subsystems is in the mitigation 
    of accident consequences. The proposed change does not allow 
    unlimited continuous operation with the plant in a condition where 
    an additional single failure could result in a loss of ECCS 
    function. The proposed change does not increase the consequences of 
    an accident because accident analysis presented in NEDC-31310P, 
    Duane Arnold Energy Center SAFER/GESTRA-LOCA Loss-of-Coolant 
    Accident Analysis, indicated that an adequate level of protection is 
    maintained by the ADS System and the remaining Operable ECCS 
    subsystems when HPCI and one RHR pump are inoperable. Therefore, 
    this change will not involve a significant increase in the 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change will not involve any physical changes to 
    plant systems, structures, or components (SSCs), or the manner in 
    which these SSCs are operated, maintained, modified, tested, or 
    inspected. The change ensures the remaining ECCS capability is 
    adequate to mitigate the consequences of accidents. Therefore, this 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluate.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change does not significantly reduce the margin of 
    safety because accident
    
    [[Page 68308]]
    
    analysis presented in NEDC-31310P, Duane Arnold Energy Center SAFER/
    GESTR-LOCA Loss-of-Coolant Accident Analysis, indicates that the 
    plant is protected by the ADS System and the remaining ECCS 
    subsystems when HPCI and one RHR pump are inoperable. The accident 
    analysis demonstrates that in this condition, the peak clad 
    temperature remains below the regulatory limit. However, with both 
    HPCI and one RHR pump inoperable, another single failure may place 
    the plant in a condition where adequate core cooling may not be 
    available during an accident. Therefore, a Completion Time of 7 days 
    has been assigned to either restore the inoperable HPCI System or 
    the RHR pump. In addition, this change provides the benefit of 
    potentially avoiding an unnecessary plant shutdown (due to a 
    Completion Time being provided for the HPCI System and one RHR pump 
    inoperable) when the remaining ECCS subsystems and the ADS are 
    capable of mitigating potential events. Therefore, this change does 
    not involve a significant reduction in a margin of safety.
    
    Condtion I
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change will allow the HPCI system and one ADS valve 
    to be inoperable for up to 72 hours. The ECCS subsystems affected by 
    this change are not assumed to be initiators or analyzed events. 
    Therefore, the proposed change does not increase the probability of 
    any accident. The role of these ECCS subsystems is in the mitigation 
    of accident consequences. The proposed change does not allow 
    unlimited continuous operation with the plant in a condition where 
    an additional single failure could result in a loss of ECCS 
    function. The proposed change does not increase the consequences of 
    an accident because accident analysis presented in NEDC-31310P, 
    Duane Arnold Energy Center SAFER/GESTER-LOCA Loss-of-Coolant 
    Accident Analysis, indicates that an adequate level of protection is 
    maintained by the remaining ADS valves (the ADS design function is 
    maintained) in combination with the remaining Operable ECCS 
    subsystems when HPCI and one ADS valve are inoperable. Therefore, 
    this change will not involve a significant increase in the 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or difference 
    kind of accident form any accident previously evaluated?
        The proposed change will not involve any physical changes to 
    plant systems, structures, or components (SSCs) or the manner in 
    which these SSCs are operated, maintained, modified, tested, or 
    inspected. The change ensures the remaining ECCS capability in 
    adequate to mitigate the consequences of accidents. Therefore, this 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change does not significantly reduce the margin of 
    safety because accident analysis presented in NEDC-31310P, Duane 
    Arnold Energy Center SAFER/GESTR-LOCA Loss-of-Coolant Accident 
    Analysis, indicates that the plant is protected by the remaining ADS 
    valves and the low pressure ECCS subsystems when HPCI and one ADS 
    valve are inoperable. The accident analysis demonstrates that in 
    this condition, the peak clad temperature remains below the 
    regulatory limit. However, with both HPCI and one ADS valve 
    inoperable, another single failure (i.e., of an ADS valve) may place 
    the plant in a condition where adequate core cooling may not be 
    available during a small or intermediate break LOCA. Therefore, a 
    Completion Time of 72 hours has been assigned to either restore the 
    inoperable HPCI System or the ADS valve. In addition, this change 
    provides the benefit of potentially avoiding an unnecessary plant 
    shutdown (due to a Completion Time being provided for the HPCI 
    System and one ADS valve inoperable) when the remaining ECCS 
    subsystems and ADS valves are capable of mitigating potential 
    events. Therefore, this change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401.
        Attorney for licensee: Jack Newman, Kathleen H. Shea, Morgan, 
    Lewis, & Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        Acting NRC Project Director: Richard P. Savio.
    
    Indiana Michigan Power Company
    
    [Docket Nos. 50-315 and 50-316]
    
    Donald C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: August 1, 1997 (AEP:NRC:0906H).
        Description of amendment requests: The proposed amendments would 
    revise Technical Specification surveillance 4.7.1.2.b. to delete the 
    requirement that the test be performed at a specified secondary steam 
    supply pressure.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1
    
        The proposed changes will not significantly increase the 
    probability or consequences of an accident previously evaluated.
        This is an administrative change intended to clarify the 
    technical specification. There will be no change to the test 
    procedure as a result of this clarification. The proposed change 
    better correlates with the accident requirements for which TDAFP 
    [turbine driven auxiliary feed pump] flow is required, and the 
    change is consistent with the present requirement of testing the 
    TDAFP at a secondary side pressure greater than 310 psig.
    
    Criterion 2
    
        The proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The proposed change does not physically modify the plant, nor does 
    it result in the installation of equipment which could introduce a 
    new failure mechanism.
    
    Criterion 3
    
        The proposed change does not involve a significant reduction in 
    a margin of safety. The proposed change does not affect the 
    performance of the TDAFP. Thus, the TDAFP remains capable of 
    providing the required flow under accident conditions, and no safety 
    margins are reduced.
        This is an administrative change intended to clarify the 
    technical specification. There will be no change to the test 
    procedure as a result of this clarification
    
        .The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Richard P. Savio, Acting.
    
    Indiana Michigan Power Company
    
    [Docket Nos. 50-315 and 50-316]
    
    Donald C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: August 11, 1997 (AEP:NRC:1265).
        Description of amendment requests: The proposed amendments would 
    revise the Technical Specifications (TS) to allow the filling of the 
    emergency core cooling system (ECCS) accumulators without declaring 
    ECCS equipment inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    [[Page 68309]]
    
    Criterion 1
    
        This amendment request does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because the proposed changes to the T/S represent the 
    possibility of an event that has such a low probability as to not be 
    considered credible. A calculation was performed that demonstrated 
    the CDF resulting from the accumulator fill line operation with all 
    of the conditions assumed above is approximately 3 x 
    10--10 per year. This is well below the NEI guidelines of 
    1 x 10-6 for acceptable risk for a given evolution. 
    Therefore, based on probabilistic considerations and the robust 
    design of the pumps, we conclude the risk associated with this 
    proposed change will not result in a significant increase in the 
    probability or consequences of a previously evaluated accident.
    
    Criterion 2
    
        The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The change does not involve a physical change to the plant, but does 
    involve a change in the plant operating configuration. The 
    possibility of a LBLOCA [large break loss of coolant accident] 
    occurring during the accumulation fill evolution has been evaluated 
    and determined to not be credible. Westinghouse has confirmed the 
    accumulator fill line was not modeled in the accident analyses due 
    to the extremely short duration of the fill operation and the 
    extremely small amount of flow that the fill line is capable of 
    passing. The overall effect this configuration would have on the 
    capability of the SI [safety injection] pump to perform its design 
    function, should a LBLOCA occur during the extremely brief window of 
    opportunity, is negligible and would not create a new type of 
    accident.
    
    Criterion 3
    
        This proposed change does not involve a significant reduction in 
    a margin of safety, as the risk from the postulated sequence of 
    events is insignificant. Additionally, engineering evaluation has 
    determined that the real response of an SI pump under the postulated 
    conditions would not be severe. The rugged construction of the 
    pumps, and the design margin built into them, are factors that 
    support the engineering judgment that the affected pump would 
    continue to operate for some time, at some capacity beyond the 
    manufacturer's design limit. As a result of exceeding the limit, the 
    pump may experience some cavitation and require additional 
    corrective maintenance, but would be expected to deliver a 
    significant fraction of its design flow.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Richard P. Savio, Acting.
    
    Niagara Mohawk Power Corporation
    
    [Docket No. 50-410]
    
    Nine Mile Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of amendment request: October 7, 1997.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TS) to change the setpoints of 
    Surveillance Requirements (SRs) 4.9.6.a, 4.9.6.f, and 4.9.6.g for the 
    refueling platform main hoist. Specifically, each refueling platform 
    crane or hoist used for handling control rods or fuel assemblies within 
    the reactor pressure vessel would be demonstrated operable by:
        a. Demonstrating operation of the overload cutoff on the main hoist 
    when the load exceeds 1600 +100/-0 pounds (rather than 1200 +50/-50 
    pounds).
        f. Demonstrating operation of the loaded interlock on the main 
    hoist when the load exceeds 700 +50/-0 pounds (rather than 485 +50/-50 
    pounds).
        g. Demonstrating operation of the redundant loaded interlock on the 
    main hoist when the load exceeds 700 +50/-0 pounds (rather than 550 
    +50/-50 pounds).
        The proposed amendment, in effect, would authorize replacement of 
    the existing triangular refueling platform mast with a round, heavier 
    mast (General Electric Model NF-500) which includes an installed 
    camera/TV system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change revises the setpoints for three TS SRs based 
    on modifications to the refueling platform mast. The new mast is 
    essentially a direct replacement for the existing mast, with the 
    exception that the new mast is approximately 400 lbs. heavier, which 
    directly affects the setpoints. No change in the frequency or manner 
    in which the surveillances are performed is proposed. Refueling 
    interlocks will continue to function as designed. No changes to the 
    methods in which plant systems are operated are required. The same 
    design criteria and standards were applied to the new mast, 
    including the seismic capability of the refueling platform with the 
    heavier mast. Therefore, none of the precursors of previously 
    evaluated accidents are affected, and no new failure modes are 
    introduced.
        Based on the additional weight of the new mast and camera/TV 
    system, the revised GESTAR [General Electric GESTAR II document 
    NEDE-24011-P-A-11-U5] criteria for fuel rod damage (more 
    conservative threshold level), the use of GE11 [9x9] fuel for the 
    bundle drop analysis, the number of damaged fuel rods has increased 
    slightly for the potential fuel handling accident. The results of 
    this increase were evaluated and dispositioned against the bounding 
    calculation to show that the current USAR [updated safety analysis 
    report] analysis bounds the revised radiological consequences which 
    remain well within the GDC [General Design Criterion] 19 and 
    10CFR[part]100 limits. The systems that are available to mitigate 
    the consequences of any accident have not been affected and are 
    still capable of performing their required functions. Therefore, 
    this change will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change revises the setpoints for three TS SRs based 
    on installation of a new refueling platform which is heavier than 
    the current mast. No change in the frequency or manner in which the 
    surveillances are performed has occurred. Refueling interlocks will 
    continue to function as designed. No changes to the methods in which 
    plant systems are operated are required. The same design criteria 
    and standards were applied to the new mast, including the seismic 
    capability of the refueling platform with the heavier mast. The 
    basic function and operation of the refueling platform is unchanged. 
    The uptravel stop and downtravel mechanical cutoff setpoints are not 
    being changed and will continue to ensure that adequate water 
    shielding is maintained. As such, the change does not introduce any 
    new failure modes or conditions that may create a new or different 
    kind of accident. Therefore, this change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed change revises three TS SR setpoints based on 
    installation of a new refueling platform mast. No change in the 
    frequency or manner in which the surveillances are performed has 
    occurred. Refueling interlocks will continue to function as 
    designed. No changes to the methods in which plant systems are 
    operated are required. The same design criteria and standards were 
    applied to the new mast, including the seismic capability of the
    
    [[Page 68310]]
    
    refueling platform with the heavier mast. The addition of a camera/
    TV system will provide enhanced visibility for fuel handling 
    activities and additional assurance that the grapple is oriented 
    over the correct fuel bundle.
        The additional weight of the new mast has been evaluated and the 
    operability requirements as described in the TS and TS Bases are 
    unchanged. The modification and revised setpoints do not change the 
    function of the refueling platform main hoist. The revised setpoints 
    will continue to assure the lifting capacity of the main hoist will 
    not be sufficient to result in damage to core internals or the 
    reactor pressure vessel in the event that they are accidentally 
    engaged.
        The necessary systems are still available to mitigate any 
    potential radiological consequences of the increased number of 
    damaged fuel rods. The radiological consequences remain within the 
    bounds of the current safety analysis and well below the GDC 19 and 
    10CFR[Part]100 limits. Therefore, the change does not involve any 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa.
    
    Niagara Mohawk Power Corporation
    
    [Docket No. 50-410]
    
    Nine Mile Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of amendment request: October 31, 1997.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TSs) to support installation of the 
    General Electric Nuclear Measurement Analysis and Control (NUMAC) Power 
    Range Neutron Monitor (PRNM) System. The TS changes apply to Sections 
    2.2, ``Limiting Safety System Settings''; 3/4.3.1, ``Reactor Protection 
    System Instrumentation'' and its corresponding Bases; and 3/4.3.6, 
    ``Control Rod Block Instrumentation.''
        Basis for proposed no significant hazards consideration 
    determination: The NUMAC-PRNM will monitor groups of Local Power Range 
    Monitor (LPRM) signals and, together with the Oscillation Power Range 
    Monitor (OPRM), initiate a reactor scram upon identifying neutron flux 
    oscillations characteristic of a thermal-hydraulic instability. The 
    NUMAC-PRNM will replace the existing Average Power Range Monitor (APRM) 
    System and will ultimately support the activation of the OPRM. The 
    proposed modification is in response to Generic Letter 94-02, ``Long-
    Term Solutions and Upgrade of Interim Operating Recommendations for 
    Thermal-Hydraulic Instabilities in Boiling Water Reactor.'' Except for 
    minor deviations, the proposed TS changes are consistent with General 
    Electric Licensing Topical Report (LTR), NEDC-32410P-A, ``Nuclear 
    Measurement Analysis and Control Power Range Neutron Monitor (NUMAC-
    PRNM) Retrofit Plus Option III Stability Trip Function,'' which was 
    approved by the NRC staff September 5, 1995. Changes with respect to 
    response time testing requirements would be based on Supplement 1 to 
    NEDC-32410P-A, approved by the NRC staff December 26, 1996.
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
    
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        As discussed in NEDC-3241OP-A, the NUMAC-PRNM modification and 
    associated changes to the TS involve systems that are intended to 
    detect the symptoms of certain events or accidents mitigating 
    actions. The worst case failure of the systems involved would be a 
    failure to initiate mitigative actions (i.e., scram or rod block), 
    but no failure can cause an accident and therefore the probability 
    of precursors of any accidents previously evaluated is not 
    increased. The NUMAC-PRNM system performs the same operations as the 
    existing equipment, reduces the need for tedious operator action 
    during normal conditions and allows the operator to focus more on 
    overall plant conditions. Automatic self-test and increased operator 
    information available with the NUMARC-PRNM system is likely to 
    reduce the burden during off-normal conditions as well. The NUMAC-
    PRNM system is compatible with the environmental conditions at the 
    mounting location (e.g., temperature, humidity, seismic, 
    electromagnetic fields) such that system performance will not be 
    degraded when compared to the system being replaced. Therefore, the 
    proposed change will not result in a significant increase in the 
    probability of any accidents previously evaluated.
        The proposed changes to the RPS [reactor protection system] and 
    Control Rod Block instrumentation TSs are necessitated by the NUMAC-
    PRNM replacement. As discussed in the evaluation, in the 4 APRM 
    channel configuration, any two of the four APRM channels and one 2-
    out-of-4 voter channel in each RPS trip system are required to 
    function for the APRM safety trip function to be accomplished. 
    Therefore, the proposed TS change requires that 3 of the 4 APRM 
    channels be operable. This assures at least two APRM channels to 
    each of the 2-out-of-4 voter channels are available in the event of 
    a single APRM channel failure and one APRM is bypassed. Also, the 
    proposed TS requires a minimum of two 2-out-of-4 voter channels per 
    RPS trip system (i.e., all four voter channels). This assures that 
    at least one voter channel per trip system is available even in the 
    event of a single voter channel failure. Surveillance testing 
    requirements were revised to take advantage of certain features of 
    the NUMAC-PRNM (digital) replacement of the existing analog APRM 
    system. These advantages included improved accuracy, stability , 
    self-testing, reduced drift, and constant time for digital 
    processing. Testing of the RPS and Control Rod Block instrumentation 
    will continue to be performed as described in the evaluation to 
    assure that the reliability and performance of these systems will 
    not be adversely affected.
        The proposed NUMAC-PRNM replacement system has been specifically 
    designed to assure that the system response times meet the current 
    acceptance limits (worst case). As a result, due to statistical 
    variations resulting from the sampling and update cycles, the 
    response time is typically faster than required in order to assure 
    the required response time is always met. The architecture of the 
    NUMAC-PRNM system has reduced segmentation compared to the existing 
    PRM system. Examples of the reduced segmentation are combining 
    previously separate functions, several input channels sharing an 
    input board, and a central loop processor for many channels. The 
    replacement equipment includes up to 5 LPRM inputs on a single 
    module compared to one per module on the current system. Up to 17 
    LPRM signals are processed through one preprocessor. The 
    recirculation flow signals are processed in the same hardware as the 
    LPRM processing. The net effect of these architectural aspects is 
    that there are some single failures that cause a greater loss of 
    ``sub-functionality'' than in the current system. However, other 
    architectural and functional aspects have an offsetting effect. 
    Redundant power supplies are used so that a single failure of AC 
    power has no effect on the overall NUMAC-PRNM system functions while 
    still resulting in a half scram, as does the current system. 
    Continuous automatic self-test also assures that if a single failure 
    does occur, it is much more likely to be detected immediately. The 
    net effect is that from a total system level, there is no increased 
    risk of loss of critical functionality or reduction in safety 
    margins due to the architecture of the replacement system.
        Failure analysis indicates that a software common cause failure 
    is not a significant contributor to the unavailability of the NUMAC-
    PRNM. However, in spite of that conclusion, means are provided 
    within the system to mitigate the effects of such a failure and 
    alert an operator. Therefore, such a failure, even if it occurred, 
    will not increase
    
    [[Page 68311]]
    
    the consequences of a previously evaluated accident. To reduce the 
    likelihood of common cause failures of software controlled 
    functions, thorough and careful verification and validation (V&V) 
    activities are performed both for the requirements and the 
    implementing software design. In addition, the software is designed 
    to limit the loading that external systems or equipment can place on 
    the system, thus significantly reducing the risk that some abnormal 
    dynamic condition external to the system can cause an overload. For 
    conservatism, however, despite, these V&V activities, common cause 
    failures of software controlled functions due to residual software 
    design faults are assumed to occur. Both the software and hardware 
    are designed to manage the consequences of such failures. Safety 
    outputs are designed to be fail safe by requiring dynamic update of 
    output modules or data signals, where failure to update the 
    information is detected by simple receiving hardware, which in turn, 
    forces a trip. This aspect covers all but rather complex failures 
    where the hardware or software executes a portion of the overall 
    logic but fails to process some portion of the new information 
    (inputs ``freeze'') or some portion of the logic (outputs 
    ``freeze''). To help reduce the likelihood of complex failures, a 
    watchdog timer is used which is updated by a very simple software 
    routine that in turn monitors the operational cycle time of all 
    tasks in the system. The software design is such that as long as all 
    tasks are updating at the design rate, it is likely that software 
    controlled functions are executing as intended. Conversely, if any 
    task fails too update at the design rate, that is a strong 
    indication of at least some unanticipated condition. If such a 
    condition occurs, its watchdog timer will not be updated, the 
    computer will be restarted, and the outputs will detect an abnormal 
    condition and provide an alarm.
        It is very difficult to quantify a software common cause failure 
    rate. Analyses for the current system did consider common cause 
    failures and assessed them to be at a rate of about 0.3 times the 
    random failure rate. The reference analysis uses a field basis for 
    the random rates. The analysis for the replacement design uses 
    conservative estimates for failure rates of equipment that are 
    actually a little higher than those assumed for the current 
    equipment. The methodology being applied concludes that the common 
    mode failure rate for the replacement system is somewhat higher than 
    the current system. However, that is offset by more frequent 
    surveillance tests performed by the self-test that result in an 
    estimated slightly lower unavailability for the NUMAC-PRNM scram 
    function compared to the current PRM system. The USAR, in general, 
    considers the failure rate of the function, not that of sub-
    components. On that basis, there will not be an increase, due to 
    software common cause failure, in the probability of a malfunction 
    analyzed in the USAR.I21The NUMAC-PRNM human-machine interface 
    design does not introduce an increased burden or constraints on the 
    operators' ability to adequately respond to an accident such that 
    there would be more severe consequential effects. The information 
    available to the operators is the same as with the current system. 
    No actions are required by the operator to obtain information 
    normally used and equivalent to that available with the current 
    equipment. However, the replacement system does provide more direct 
    accessible information regarding the condition of the equipment, 
    including automatic self-test, which can aid the operator in 
    diagnosing unusual situations beyond those defined in the licensing 
    basis.
        The replacement system has a significantly lower power 
    requirement and is generally smaller, reducing somewhat the seismic 
    loading on the panels. The equipment qualification also includes EMI 
    [electro magnetic induction] emissions which, combined with the fact 
    that the replacement equipment is mounted in its own cabinet 
    (replaces all of the current equipment), minimized the likelihood of 
    significant impact on other existing equipment.
        The replacement equipment makes increased use of qualified 
    optical methods to provide both safety and functional isolation 
    between safety-related and nonsafety-related systems. Where fiber 
    optic methods cannot be used, the isolation provided is comparable 
    to or better than that provided in the current system.
        The net electrical and thermal load for the replacement system 
    is less than that for the current system. Accordingly, the 
    replacement system had adequate cabinet cooling and no forced 
    cooling is required.
        The replacement system meets or exceeds all applicable 
    requirements for separation, independence and grounding. The use of 
    fiber optic connections between the APRM and RBM [rod block monitor] 
    improves the separation and reduces the dependence of the system on 
    common grounds. However, for noise rejection, the equipment design 
    and manufacturing requirements assure improved grounding of the 
    actual equipment.
        No change in wiring or grounding external to the panels 
    containing the replacement equipment is necessary for correct 
    operation of the replacement equipment.
        NEDC-3241OP-A, Section 3.2.3, discusses different plant 
    configurations for recirculation flow channels, including the case 
    where plants currently (before implementing the NUMAC PRNM system) 
    have four flow channels. Absence of any discussion in the LTR 
    related to separation for plants originally having four flow 
    channels implies that those plants are expected to meet full 
    separation requirements. The LTR includes a further statement that 
    ``The criterion is to maintain equal or better protection against 
    single failures while allowing bypassing of the APRM channel that 
    processes the flow signal.''
        The NMPC [Niagara Mohawk Power Corporation] NUMAC PRNM system 
    has four recirculation low channels, but the flow input circuits for 
    two of the four are not separated from each other outside the PRNM 
    panel. As a result, a single failure that causes both of these flow 
    signals to go high could, depending on the specific value, cause the 
    APRM flow biased trip setpoint in two channels to go to the clamped 
    setpoint. If, at the same time, a third channel is bypassed, the 
    APRM flow-biased trip setpoint for the APRM system could be non-
    conservative. (NOTE: The flow signals are compared to one another. 
    Should the flow signals not be within specified limits, an alarm and 
    a control rod block would be initiated.)
        Despite the fact that two of the four flow input circuits are 
    not separated from each other outside the PRNM panel, the 
    replacement system is judged to be adequate with the current field 
    routing of flow signals and meets the LTR criteria. This conclusion 
    is based on the fact that there is no credible fault in the circuits 
    within the duct, in which the flow signals are routed, that can 
    damage the other circuits. Also, there is no credible external fault 
    that can damage the circuits inside the duct. Therefore, it is 
    concluded that the separation between the two flow input circuits is 
    adequate to meet the system single failure requirements in that no 
    credible single failure will disable the flow inputs to more than 
    one APRM channel. Additionally, there are no reload licensing 
    transient analyses that take credit for the flow-biased simulated 
    thermal power scram setpoint.
        The replacement design has been specifically designed to have 
    the same or more conservative ``fail safe'' failure modes as the 
    current system. For example, in the case of a single power bus 
    failure, the current system loses about one half of the LPRM 
    information and an output trip occurs. For the replacement system, 
    that failure still results in an output trip, but no LPRM 
    information is lost. In the current system, a static failure in 
    several areas in the system could result in a ``fail-as-is'' state 
    of the outputs. In the replacement system, dynamic coupling starting 
    in the main processor and going to the final output virtually 
    eliminates ``fail-as-is'' failure modes and replaces them with 
    ``fail tripped'' modes.
        The replacement system has the same loss of power failure mode 
    as the current system relative to the trip outputs and for loss of 
    AC [alternating current] power. For loss of DC [direct current] 
    power, the replacement system in most cases continues to operate 
    normally due to redundancy of the power supplies. Therefore, the 
    consequences are no different or improved compared to those 
    considered in the USAR.
        Both the current system and the replacement system automatically 
    startup on application of power (or re-application). However, the 
    replacement system may take slightly longer to reach normal 
    operation due to initializing activities. However, no USAR 
    evaluations take credit for rapid start of the PRM. Therefore, the 
    slightly longer startup time from point of power application is 
    bounded by the USAR analysis. Upon application of power, once the 
    system is set up for the specific application, it automatically 
    returns to those settings upon application of power. All such setup 
    parameters are stored in non-volatile memory.
        Human-machine interfaces (HMI) failures in the current system 
    could be related to misadjusted settings, incorrect reading of 
    meters, and failure to return the equipment to the normal operating 
    configuration. There are comparable failure modes for some of these 
    in the digital system where an
    
    [[Page 68312]]
    
    erroneous potentiometer adjustment in the current system is 
    equivalent to an erroneous digital entry in the replacement system. 
    Certain potential ``failure to reconfigure'' errors in the current 
    system have no counterpart in the replacement system because any 
    ``reconfiguration'' is automatically returned to normal by the 
    system. Also, since parameters are available for review at any time, 
    even if an error such as a digital entry error occurs, it is more 
    likely that the error would be almost immediately detected by 
    recognition that the displayed value is not the correct one. Failure 
    analysis of the current system assumes certain rates of human error. 
    The rates for the replacement system will be lower, and hence are 
    bounded by the USAR analysis. The NUMAC-PRNM system has been 
    approved as an acceptable neutron monitoring replacement by the NRC.
        Therefore, based on the above discussions, the proposed change 
    will not result in a significant increase in the consequences of any 
    accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        NMPC proposes to replace the existing RPS APRM system with the 
    NUMAC-PRNM system and make associated changes to the RPS and Control 
    Rod Block TS instrumentation sections. As discussed in NEDC-3241OP-
    A, no new system level failure modes are created with the 
    replacement system. The NUMAC-PRNM modification and associated 
    changes to the TSs involve systems that are intended to detect the 
    symptoms of certain events or accidents and initiate mitigating 
    actions. The worst case failure of the systems involved would be a 
    failure to initiate mitigative actions (i.e., scram or rod block), 
    but no failure can cause an accident. This is unchanged from the 
    current system. The proposed changes do not modify the basic 
    functional requirements of the affected equipment, create any new 
    system interfaces or interactions nor create any new system failure 
    modes or sequence of events that could lead to an accident. The 
    replacement system is more tolerant of degraded power than the 
    current system. Software common cause failures can at most cause the 
    system to fail to perform its safety function. As with system level 
    failures, software failures could fail to initiate actions to 
    mitigate the consequences of an accident, but would not cause one. 
    Surveillance testing will continue to be performed to assure 
    reliability and maintain current performance levels.
        The NUMAC-PRNM system is a digital system with software 
    (firmware) control. As such, it has ``central'' processing points 
    and software controlled digital processing where the current system 
    has analog and discrete component processing. The result is that the 
    specific failures of hardware and potentially common cause software 
    are different from the current system. Also, automatic self-test 
    results in some cases in a direct trip as a result of a hardware 
    failure where the current system may have remained ``as is.'' 
    However, when these are evaluated at the system level, there are no 
    new effects. In general, the USAR assumes simplistic failure modes 
    (relays for example) but does not specifically evaluate effects 
    added by the NUMAC-PRNM such as self-test detection and automatic 
    trip or alarm. The effects of software common cause failures are 
    mitigated by hardware design and system architecture. The 
    replacement system is fully qualified to operate in its installed 
    location and will not affect other equipment. The NUMAC-PRNM system 
    has been approved as an acceptable neutron monitoring replacement by 
    the NRC. Therefore, the proposed change will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed modification and associated TS changes will not 
    adversely affect the performance characteristics of the RPS and 
    Control Rod Block instrumentation nor will it affect the ability of 
    the subject instrumentation to perform its intended function. As 
    stated in NEDC-3241OP-A, the replacement system has improved channel 
    trip accuracy compared to the current system and meets or exceeds 
    system requirements assumed in setpoint analysis. Also, the channel 
    response time is within acceptable limits, the channel indicated 
    accuracy is improved over the current system, and the replacement 
    system does not cause a plant parameter for any analyzed event to 
    fall outside of acceptable limits. The surveillance testing and 
    frequencies proposed will assure reliability of the RPS and Control 
    Rod Block instrumentation. In addition, the subject equipment was 
    qualified, where appropriate, to assure its intended safety function 
    is performed. Therefore, the proposed changes do not involve 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: S. Singh Bajwa.
    
    Pacific Gas and Electric Company
    
    [Docket Nos. 50-275 and 50-323]
    
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo 
    County, California
    
        Date of amendment requests: July 30, 1997.
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant Unit Nos. 1 and 2 to add a limiting condition for operation 
    and surveillance requirements for a residual heat removal (RHR) pump 
    trip on low refueling water storage tank (RWST) level to TS 3/4.3.2, 
    ``Engineered Safety Features Actuation System Instrumentation.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This change assures the availability of the refueling water 
    storage tank (RWST) low-level trip of the residual heat removal 
    (RHR) pumps by establishing limits on the time that a channel can be 
    out of service to 72 hours and establishing surveillance criteria to 
    verify the operation of the logic. The RHR system is used to respond 
    to loss of coolant accidents (LOCAs) and other (e.g., secondary 
    side) accidents that could result in initiation of a safety 
    injection signal, and is not a precursor to any of these events as 
    evaluated in safety analyses. Under accident conditions the RWST 
    serves as the source of water for the emergency core cooling system 
    (ECCS) pumps and the containment spray pumps. The RWST and the RHR 
    pump trip are accident mitigation components and are not precursors 
    for any accident evaluated in the safety analyses.
        The existing Technical Specification (TS) would allow one RWST 
    level indication channel to be inoperable indefinitely, and has an 
    allowed outage time (AOT) for two channels inoperable of up to seven 
    days. Additionally, the existing TS does not apply to the RWST low-
    level RHR pump trip logic. The new TS provides controls that require 
    that all three RWST low-level trip channels be maintained operable 
    while the plant is in Modes 1 to 4, and provides for an AOT for one 
    channel inoperable for up to 72 hours, if the inoperable channel is 
    placed in the cut-out mode within 6 hours. By placing the inoperable 
    channel in the cut-out mode, the possibility of a channel failure 
    causing an RHR pump failure to start at the onset of an accident is 
    precluded even with a single active failure. This assures that the 
    consequences of an accident are not increased.
        The change will have no affect on the probability of a physical 
    failure of an RHR pump because it only ensures the presence of a 
    pump trip signal when required. Therefore, there is no increase in 
    the probability of failure of an RHR train to function as designed. 
    This change will have no affect on the probability of any other ECCS 
    equipment failure as it only affects the presence of a trip signal 
    for the RHR pumps.
    
    [[Page 68313]]
    
        The new TS 3.3.2 item would provide controls that require that 
    all three RWST level channels be maintained operable while the plant 
    is in operating Modes 1 to 4 (power operation through hot shutdown). 
    By maintaining the three channels operable, the RHR pump actuation/
    trip logic operability is assured so that the RHR and RWST can in 
    all cases perform their intended accident mitigation functions 
    following a design basis event as evaluated in the safety analyses.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The RHR system is used to respond to LOCAs and other (e.g., 
    secondary side) accidents that could result in initiation of a 
    safety injection signal. Under accident conditions the RWST serves 
    as the initial source of water for injection by the RHR and other 
    ECCS pumps, and is the source of water for the containment spray 
    pumps. This change does not affect operation of the systems as it 
    relates to their response to accident conditions. It provides 
    additional assurance that the RHR pump trip logic will operate as 
    designed by establishing administrative controls on the time the 
    system is susceptible to a single failure. No new failure modes have 
    been introduced.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The relevant margin of safety is based on the RHR pumps starting 
    and then automatically stopping at the correct RWST water level. The 
    new TS 3.3.2 item provides controls that require all three RWST 
    level channels be maintained operable while the plant is in Modes 1 
    to 4. By maintaining the three channels operable, the capability of 
    the RHR pump actuation/trip logic to survive a single active failure 
    is assured. Therefore, the trip logic operability is assured and the 
    margin is preserved. This change also provides additional assurances 
    that the remaining water in the RWST at the time of switchover is 
    consistent with that assumed in the Final Safety Analysis Report and 
    Safety Evaluation Reports.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Richard F. Locke, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: William H. Bateman.
    
    Pennsylvania Power and Light Company
    
    [Docket Nos. 50-387 and 50-388]
    
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: June 25, 1997.
        Description of amendment request: The amendments would modify the 
    Susquehanna Steam Electric Station, Units 1 and 2 Technical 
    Specifications to reflect an increase in the secondary containment 
    bypass leakage. Specifically, Section 3.6.1.2 is changed to replace the 
    leakage of 1.2 scf per hour for any one main steam line drain with 
    25.43 scfh for secondary containment bypass leakage from all sources; 
    Section 3.6.1.2 is changed to include the Main Steam Line Drain, high-
    pressure coolant injection (HPCI) system drain, and reactor core 
    isolation cooling (RCIC) system drain leakages as part of the 300 scfh 
    leakage requirement; and Section 3/4.6.1.2 is changed to include a 
    discussion which related the secondary containment bypass leakage TS to 
    the radiological dose analyses.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Of the potential accidents described in FSAR [Final Safety 
    Analysis Report] Chapters 6 and 15, only a ``Decrease in Reactor 
    Coolant Inventory'' as described in FSAR Section 15.6.5 is affected 
    by the proposed action. The specific accident of concern is a design 
    basis LOCA [loss-of-coolant accident] concurrent with a LOOP [loss-
    of-offsite power] which results in RPV [reactor pressure vessel] 
    depressurization and failure to recover RPV level above the FW 
    [feedwater] spargers. For this accident, the current licensing basis 
    offsite and control room dose analyses assume a secondary 
    containment bypass leakage rate of 9 scfh and primary containment 
    water (called ESF [engineered safety function]) leakage of 5 gpm. 
    The current licensing basis analyses do not attribute this leakage 
    to any specific pathway.
        The proposed action does not increase the probability of a 
    previously analyzed accident in any way. The condition of concern is 
    the result of an accident and as such does not contribute to the 
    initiation of an accident as analyzed in the FSAR.
        Of concern is whether or not the proposed action significantly 
    increases the consequences of an accident as previously evaluated. 
    Calculations of off-site dose assuming SCBL [secondary containment 
    bypass leakage] of 28 scfh, primary containment water leakage of 20 
    gpm, and crediting suppression pool scrubbing show decreases in 
    thyroid dose, but slight increases in whole body dose when compared 
    with dose calculations performed to support the removal of the MSIV-
    LCS [main steam isolation valve-leakage control system]. This result 
    is expected because the effect of suppression pool scrubbing is 
    factored into the revised licensing basis analysis. Suppression pool 
    scrubbing is effective in reducing iodine release but has no assumed 
    effect on the removal of noble gases. Since the methodology/
    assumptions for scrubbing are acceptable to the NRC [Nuclear 
    Regulatory Commission] per the guidance in SRP [Standard Review 
    Plan] Section 6.5.5 and the values for decontamination factors are 
    conservative, the judgment may be made that considerable margin is 
    preserved within the analysis.
        Although the whole body dose with SCBL of 28 scfh and water 
    leakage of 20 gpm is increased from the previously approved MSIV-LCS 
    dose analysis, the increase is small (about 1 rem at the two hour 
    site boundary; less than 0.1 rem 30 day LPZ [low population zone]). 
    The total dose including the increase is still well below the 
    10CFR100 whole body regulatory limit of 25 rem to which SSES 
    [Susquehanna Steam Electric Station] was licensed. No change in 
    operating procedures is anticipated. Calculated post accident 
    control room thyroid dose decreases as a result of this change, and 
    the increase in control room whole body dose is less than 0.05 rem, 
    well below the 10CFR50, Appendix A, GDC [General Design Criterion] 
    19 dose limits outlined in NUREG-0800. Thus, no appreciable effect 
    on operator response will occur as a result of this change.
        The addition of the HPCI and RCIC Steam Line Drains to the Tech 
    Spec for MSIV leakage is being performed as a result of the 
    modification which eliminated the MSIV Leakage Control System (MSIV 
    LCS). At the time this modification was performed, these lines were 
    not identified as potential SCBL pathways. However, because leakage 
    from the HPCI and RCIC drain lines are part of the same pathway to 
    the condenser which is now used by the main steam line drains (MSLD) 
    and included in the Technical Specifications, they must be combined 
    with the MSIV's and MSLD to be less than 300 scfh. This change only 
    affects the accounting of the various drain leakages in the valve 
    testing program. The justification for this change is the same 
    justification provided in the ITS [Improved Technical Specification] 
    submittal (PLA-4488, August 1, 1996) which adds the MSLD to this 
    Technical Specification. The test pressure change to allow testing 
    at Pa was previously proposed in PLA-4502, September 23, 1996. One 
    additional change to delete a footnote related to the removal of the 
    MSIV Leakage Control System is
    
    [[Page 68314]]
    
    included because this system has been removed from Susquehanna SES.
        Since the increase in SCBL and primary containment water leakage 
    result in only a small increase in the doses previously evaluated by 
    the NRC and the other changes do not affect the dose analyses, the 
    proposed change does not result in a significant increase in the 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Because the FSAR analysis already assumes SCBL and ESF leakage 
    occur and the other changes do not affect the type of accident[s] 
    that are postulated to occur, the proposed change does not present 
    the possibility of an accident of a different type. Additionally, 
    the change in dose analysis methodology does not create an accident 
    or malfunction of a different type since it only involves the 
    analysis of the effects of such accidents or malfunctions.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        This question addresses changes in system parameters only. Dose 
    consequences are addressed in Section 1 above. The only Technical 
    Specification dealing with SCBL is T.S. 3.6.1.2 which requires the 
    leakage from any one Main Steam Line Drain (MSLD) Valve to be less 
    than or equal to 1.2 scfh when tested at Pa (45.0 psig). As noted 
    earlier, the current licensing basis accident dose analysis assumes 
    a total of 9 scfh for bypass leakage and 5 gpm for primary 
    containment water leakage but does not attribute them to any 
    particular source. The proposed action increases the assumed SCBL 
    from 9 to 28 scfh and water leakage from 5 gpm to 20 gpm. These 
    leakage rates are insignificant in terms of SGTS [standby gas 
    treatment system] flows or water loss from ECCS systems. These 
    leakage rates do not affect building temperatures or pressures so 
    that they become closer to acceptance limits. Likewise, no other 
    system parameter values become closer to limits as a result of these 
    changes in leakage. Consequently, the existing margin of safety 
    between the licensing basis analysis and system parameter acceptance 
    limits is not reduced. The changes to the HPCI, RCIC, and main steam 
    line drain leakage only affect the accounting for the various 
    leakages in the leakage testing program. The deletion of the 
    footnote is administrative because the MSIV Leakage Control System 
    has been removed from the Susquehanna SES. The change in test 
    pressure was previously evaluated in PLA-4502, September 23, 1996. 
    Thus, no decrease in margin of safety results.
    
        The NRC staff has reviewed the licensee's analysis and notes that a 
    discussion of the administrative change to delete a footnote in Section 
    3.6.1.2 is in the third section of the no significant hazards 
    consideration. The staff finds that this administrative change also 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated and does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated. Based on this staff review, it appears 
    that the three standards of 10 CFR 50.92(c) are satisfied. Therefore, 
    the NRC staff proposes to determine that the amendment request involves 
    no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company
    
    [Docket No. 50-387]
    
    Susquehanna Steam Electric Station, Unit 1, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 26, 1997.
        Description of amendment request: The amendment would modify the 
    Susquehanna Steam Electric Station, Unit 1 Technical Specifications to 
    change the definitions in Section 1.0 to make them applicable to 
    ATRIUM-10 fuel (reflecting the new design), to include the Unit 1 Cycle 
    11 flow dependent minimum critical power ratio (MCPR) Safety Limits in 
    Sections 2.1.2 and 3.4.1.1.2, to change Section 5.3.1 to reflect the 
    ATRIUM-10 design, and to include Siemens Power Corporation methodology 
    topical reports and references to the methodology in Section 6.9.3.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The applicable sections of the FSAR [Final Safety Analysis 
    Report] are Chapters 5, 6.3, 9, and 15 of the FSAR. Chapter 5 
    discusses the results of the ASME [American Society of Mechanical 
    Engineers] overpressure analysis for the reactor pressure boundary. 
    Chapter 6.3 discusses the LOCA [loss-of-coolant accident]. Chapter 9 
    discusses fuel storage and handling. Chapter 15 describes the 
    transient and accident analyses, a majority of which have been 
    dispositioned to be non-limiting. A discussion of the impact of the 
    Technical Specification changes is provided below.
        The change to Definitions 1.2 and 1.3 makes the definitions 
    applicable to ATRIUM TM-10. There are no effects on 
    safety functions from this change.
        A cycle specific MCPR Safety Limit analysis was performed for 
    PP&L [Pennsylvania Power and Light Company] by SPC [Siemien Power 
    Corporation]. This analysis used NRC [Nuclear Regulatory Commission] 
    approved methods described in Technical Specification Reference 13 
    (ANF-524(P)(A), Revision 2 and Supplement 1 Revision 2), as modified 
    by EMF-97-010(P), Rev. 1. The SAFETY LIMIT MCPR calculation 
    statistically combines uncertainties on feedwater flow, feedwater 
    temperature, core flow, core pressure, core power distribution, and 
    the uncertainty in the Critical Power Correlation. The SPC analysis 
    used cycle specific power distributions and calculated MCPR values 
    such that at least 99.9% of the fuel rods are expected to avoid 
    boiling transition during normal operation or anticipated 
    operational occurrences. The SAFETY LIMIT MCPRs are specified as a 
    function of core flow. The resulting two-loop and single-loop values 
    (Technical Specification Sections 2.1.2 and 3.4.1.1.2) are included 
    in the proposed change. Thus, the cladding integrity and its ability 
    to contain fission products are not adversely affected.
        The MCPR methodology for ATRIUM TM-10 fuel (SPC 
    report EMF-97-010(P), Rev. 1), included in the revised Technical 
    Specifications via reference (Section 6.9.3.2) and previously 
    approved by the NRC for Unit 2 Cycle 9, describes conservative 
    methods for developing the MCPR Safety Limits and Operating Limits 
    for the U1C11 reload of ATRIUM TM-10 fuel in the 
    Susquehanna Steam Electric Station. This methodology conservatively 
    accounts for a flow dependence in the ATRIUM TM-10 
    critical power test data as well as an increased correlation 
    uncertainty for high local peaking factor rods. The results of using 
    this methodology are core flow dependent MCPR Safety Limits plus 
    conservative MCPR Operating Limits for Unit 1 Cycle 11. The 
    resulting MCPR Safety Limits and Operating Limits will continue to 
    assure that at least 99.9% of the fuel rods are expected to avoid 
    boiling transition during normal operation or anticipated 
    operational occurrences. Thus, the cladding integrity and its 
    ability to contain fission products are not adversely affected. The 
    proposed change in MCPR methodology does not physically affect the 
    plant or its systems.
        Using the approach discussed in EMF-97-010(P), Rev. 1, analyses 
    of the Pump Seizure accident with the new MCPR methodology (SPC 
    report EMF-97-010(P), Rev. 1) will demonstrate that the NRC 
    acceptance criterion (i.e., small fraction of 10CFR100 dose limits) 
    is met.
        The change to the Design Features (Section 5.3) increases the 
    maximum allowable lattice average enrichment. Analyses have 
    demonstrated that the ATRIUM TM-10 fuel will remain 
    subcritical (k-effective < 0.95)="" in="" both="" the="" spent="" fuel="" pool="" and="" the="" new="" fuel="" vault.="" thus,="" the="" change="" to="" maximum="" allowable="" lattice="" average="" enrichment="" has="" no="" impact="" on="" safety="" functions.="" the="" description="" [[page="" 68315]]="" of="" a="" fuel="" assembly="" (section="" 5.3)="" is="" also="" revised="" to="" reflect="" the="" atrium="">TM-10 central water channel, and reference to an 
    active fuel length of 150 inches was deleted. This change reflects 
    the physical characteristics of the ATRIUM TM-10 fuel and 
    has no impact on the probability or consequences of an event.
        Included in the revised Technical Specifications via reference 
    (Section 6.9.3.2) are additional NRC approved methodology reports. 
    The NRC approved topical reports contain methodology which is used 
    to assure safe operation of Unit 1 with ATRIUM TM-10 
    fuel. These methodologies assure that the core meets appropriate 
    margins of safety for all expected plant operational conditions 
    ranging from refueling and cold shutdown of the reactor through 
    power operation. Thus, the results obtained from the analyses will 
    provide assurance that the reactor will perform its design safety 
    function during normal operation and design basis events.
        The BASES changes for Section 2.1.1 (THERMAL POWER, Low Pressure 
    or Low Flow) reflect that the Safety Limit is valid for both 9x9-2 
    and ATRIUM TM-10. BASES for Section 2.1.2 were changed to 
    refer to Section 6.9.3.2 for applicable references.
        Therefore, the proposed action does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The changes to the Unit 1 Technical Specifications (Definitions, 
    MCPR safety limits, Design Features, and inclusion of methodology 
    references) to allow use of ATRIUM TM-10 fuel do not 
    require any physical plant modifications, physically affect any 
    plant components, or entail significant changes in plant operation. 
    Thus, the proposed change does not create the possibility of a 
    previously unevaluated operator error or a new single failure. The 
    consequences of transients and accidents will remain within the 
    criteria approved by the NRC. Therefore, the proposed change does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The applicable Technical Specification Sections include 1.0, 
    2.0, 3/4.4, 5.3, and 6.9.3.2.
        The changes to the Unit 1 Technical Specifications discussed in 
    Item 1 above do not require any physical plant modifications, 
    physically affect any plant components, or entail significant 
    changes in plant operation. Therefore, the proposed change will not 
    jeopardize or degrade the function or operation of any plant system 
    or component governed by Technical Specifications. The consequences 
    of transients and accidents will remain within the criteria approved 
    by the NRC. The proposed MCPR Safety Limits and the NRC approved 
    methods and revised MCPR methodology detailed in the references 
    added to Section 6.9.3.2 maintain an equivalent margin of safety as 
    defined in the BASES of the applicable Technical Specification 
    sections.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Southern California Edison Company, et al.
    
    [Docket Nos. 50-361 and 50-362]
    
    San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California
    
        Date of amendment requests: June 18, 1997.
        Description of amendment requests: The licensee proposes to revise 
    Technical Specification (TS) 3.8.1, ``AC Sources--Operating'' and 
    applicable Bases. This change will more clearly reflect safety analysis 
    and testing conditions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change would revise Technical Specification (TS) TS 
    3.8.1, ``AC Sources--Operating,'' Surveillance Requirement (SRs) 
    3.8.1.1, 3.8.1.2, 3.8.1.7, 3.8.1.10, 3.8.1.11, 3.8.1.12, 3.8.1.13, 
    3.8.1.14, 3.8.1.15, 3.8.1.16, 3.8.1.17, 3.8.1.19, and 3.8.1.20 and 
    applicable Bases to more clearly reflect surveillance test 
    conditions and system design requirements. Changes to the SRs 
    include more restrictive voltage and frequency acceptability limits. 
    The new requirements reflect the system design requirements in order 
    to ensure Class 1E system operability, meet the requirements of the 
    safety analysis, and to agree with the existing test surveillances.
        In addition, the discussion regarding design basis reactive 
    power loading is eliminated since this cannot be readily controlled 
    during testing.
        Operation of the facility would remain unchanged as a result of 
    the proposed change and no assumptions or results of any accident 
    analyses are affected. Therefore, the proposed change will not 
    involve a significant increase in the probability or consequences of 
    any accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change would revise Technical Specification (TS) TS 
    3.8.1, ``AC Sources--Operating,'' Surveillance Requirement (SRs) 
    3.8.1.1, 3.8.1.2, 3.8.1.7, 3.8.1.10, 3.8.1.11, 3.8.1.12, 3.8.1.13, 
    3.8.1.14, 3.8.1.15, 3.8.1.16, 3.8.1.17, 3.8.1.19, and 3.8.1.20 and 
    applicable Bases to more clearly reflect surveillance test 
    conditions and system design requirements.
        Operation of the facility would remain unchanged as a result of 
    the proposed change. Therefore, the proposed change will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change would revise Technical Specification (TS) TS 
    3.8.1, ``AC Sources--Operating,'' Surveillance Requirement (SRs) 
    3.8.1.1, 3.8.1.2, 3.8.1.7, 3.8.1.10, 3.8.1.11, 3.8.1.12, 3.8.1.13, 
    3.8.1.14, 3.8.1.15, 3.8.1.16, 3.8.1.17, 3.8.1.19, and 3.8.1.20 and 
    applicable Bases to more clearly reflect surveillance test 
    conditions and system design requirements. Changes to the SRs 
    include more restrictive voltage and frequency acceptability limits. 
    The new requirements reflect the system design requirements in order 
    to ensure Class 1E system operability, meet the requirements of the 
    safety analysis, and to agree with the existing test surveillances.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    Southern California Edison Company, et al.
    
    [Docket Nos. 50-361 and 50-362]
    
    San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California
    
        Date of amendment requests: November 14, 1997 (supersedes February 
    1, 1994, amendment request).
    
    [[Page 68316]]
    
        Description of amendment requests: The licensee proposes to revise 
    the licensing basis as described in the Updated Final Safety Analysis 
    Report Section 3.5, ``Missile Protection,'' to allow the use of NUREG-
    0800, ``Standard Review Plan'' methodology in evaluating tornado-
    generated missiles. In particular, a probability based criteria is 
    proposed to evaluate missile barrier requirements consistent with 
    Section 3.5.1.4 of NUREG-0800.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        NUREG-0800, Standard Review Plan (SRP) Section 3.5.1.4, Revision 
    0 and Section 3.5.1.5 Revision 1 provide a conservatively acceptable 
    probability threshold for safety due to damage caused by postulated 
    missile strikes. Section 3.5.1.4, Revision 0 uses 10-7 
    per year for a tornado-generated missile strike, and Section 3.5.1.5 
    Revision 1 uses 10-7 per year for exceeding 10 CFR Part 
    100 limits.
        The proposed criteria of probability of damage to critical 
    exposed equipment (as defined in San Onofre Updated Final Safety 
    Analysis Report proposed Table 3.5-13) of 10-7 per year 
    per unit is consistent with this guidance.
        The probability of damage to exposed critical components due to 
    a postulated missile strike of 10-7 is so small as to be 
    negligible. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This amendment request establishes a conservative criteria for 
    tornado-generated missiles consistent with the SRP guidance and will 
    not create a new or different kind of accident from any accident 
    that has been previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        This proposed change is consistent with the methodology and 
    acceptance criteria of the SRP, and the SRP criteria ensures that 
    there will be no undue risk to the health and safety of the public. 
    Therefore, there will be no significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
        Attorney for licensee: T.E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia
    
    Vogtle Electric Generating Plant, Units 1 and 2, Burke County, Georgia
    
    [Docket Nos. 50-424 and 50-425]
    
        Date of amendments request: August 8, 1997, as supplemented October 
    10, 1997. This application and supplement supersedes the October 4, 
    1996, application, noticed in the Federal Register on November 19, 1996 
    (61 FR 58903), in its entirety.
        Description of amendments request: The proposed amendments would 
    change the Technical Specifications to credit soluble boron in the 
    spent fuel pool for maintenance of subcriticality and increase the 
    allowable fuel enrichment to 5.0 percent U-235 as follows:
    
    1. Revisions to the Table of Contents
    
        The Table of Contents would be revised to include two additional 
    Technical Specifications 3.7.17, ``Fuel Storage Pool Boron 
    Concentration,'' and 3.7.18, ``Fuel Assembly Storage in the Fuel 
    Storage Pool'' and add Figures 3.7.18-1, 3.7.18-2, and 4.3.1-1 
    through 4.3.1-9 describing burnup credit, checkerboard 
    configurations and interface requirements. These changes would be 
    added to support crediting soluble boron in the fuel storage pool 
    criticality analyses.
    
    2. Addition of Technical Specifications 3.7.17 and 3.7.18
    
        Technical Specifications 3.7.17, ``Fuel Storage Pool Boron 
    Concentration,'' and 3.7.18, ``Fuel Assembly Storage in the Fuel 
    Storage Pool,'' would be added to credit soluble boron in the fuel 
    storage pool criticality analyses, and specify acceptable 
    enrichment-burnup combinations for storage of fuel in the fuel 
    storage pool.
    
    3. Revision to Technical Specification 4.3.1.1
    
        Design Features Section 4.3.1.1 would be revised to reflect the 
    increased maximum enrichment assumed in the fuel storage pool 
    criticality analyses, add a requirement to maintain Keff 
    less than 1.0 when fully flooded with unborated water, change the 
    0.95 Keff requirement from ``if fully flooded with 
    unborated water'' to ``when fully flooded with water borated to 450 
    ppm (Unit 1) or 500 ppm (Unit 2),'' and to add a reference to 
    Specification 3.7.18 for allowable enrichment-burnup combinations. 
    Requirements for fuel that do not meet the requirements of 
    Specification 3.7.18, would also be added to Section 4.3.1.1, 
    including Figures 4.3.1-1 through 4.3.1-9 depicting acceptable 
    enrichment-burnup requirements and checkerboard configurations.
    
    4. Revisions to the Table of Contents (Bases)
    
        The Table of Contents would be revised to include two additional 
    Technical Specification Bases Sections B 3.7.17 ``Fuel Storage Pool 
    Boron Concentration'' and B 3.7.18 ``Fuel Assembly Storage in the 
    Fuel Storage Pool.''
    
    5. Addition of Bases for Technical Specifications 3.7.17 and 3.7.18
    
        Two additional Technical Specification Bases Sections B 3.7.17, 
    ``Fuel Storage Pool Boron Concentration'' and B 3.7.18, ``Fuel 
    Assembly Storage in the Fuel Storage Pool'' would be added to credit 
    soluble boron in the fuel storage pool criticality analyses.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The radiological consequences of 5.0 weight percent U-235 fuel 
    on accidents previously evaluated in the Vogtle FSAR [Final Safety 
    Analysis Report] are not significant. Increasing the enrichment up 
    to and including 5.0 weight percent U-235 has minor effects on the 
    radiological source terms and subsequently the potential releases 
    both normal and accidental are not significantly affected. 
    Evaluations performed (WCAP-12610-P-A, Reference 5 [of the 
    licensee's application]) considered the source term, gap fraction, 
    and the accident doses for a maximum fuel enrichment of 5.0 weight 
    percent U-235. It was concluded that operating with and storing fuel 
    with 5.0 weight percent U-235 enrichment may result in minor changes 
    in the normal annual releases of long half-life fission products 
    that are not significant. Also, the radiological consequences of 
    accidents are minimally affected due to the very small changes in 
    the core inventory and the fact that the currently assumed gap 
    fractions remain bounding.
        The use of the slightly higher enrichment for VEGP [Vogtle 
    Electric Generating Plant] fuel will not result in burnups in excess 
    of those currently allowed for VEGP. The cycle design methods and 
    limits will remain the same as are currently licensed. Therefore, 
    the use of fuel with the higher enrichment will not result in 
    conditions outside those currently allowed for VEGP.
        There is no increase in the probability of a fuel assembly drop 
    accident in the fuel storage pool when considering the presence of 
    soluble boron in the pool water for criticality control. The 
    handling of the fuel assemblies in the fuel storage pool has always 
    been performed in borated water.
        Fuel assembly placement will be controlled pursuant to approved 
    fuel
    
    [[Page 68317]]
    
    handling procedures and will be in accordance with the spent fuel 
    rack storage configuration limitations in the Technical 
    Specifications. The consequences of a misplaced assembly have been 
    included in the analysis supporting this revision to the Technical 
    Specifications.
        There is no increase in the consequences of the accidental 
    misloading of a fuel assembly into the fuel storage pool racks 
    because criticality analyses demonstrate that the pool will remain 
    subcritical following an accidental misloading of an assembly. There 
    are no credible dilution events that reduce the subcriticality 
    margin below the 5% margin recommended in NRC guidance (references 
    1, 2, and 3 [of the licensee's application]). Even if the fuel 
    storage pool were diluted to a boron concentration of 0 ppm the No 
    Soluble Boron 95/95 analysis demonstrates that the pool will remain 
    subcritical. The proposed Technical Specifications limitations will 
    ensure that an adequate fuel storage pool boron concentration will 
    be maintained.
        There is no increase in the probability of the loss of normal 
    cooling to the fuel storage pool water due to the presence of 
    soluble boron in the pool water for subcriticality control, because 
    a concentration of soluble boron similar to the proposed limit has 
    always been maintained in the fuel storage pool water.
        The loss of normal cooling to the fuel storage pool will cause 
    an increase in the temperature of the fuel storage pool water. This 
    will cause a decrease in water density which would normally result 
    in an addition of negative reactivity. However, since Boraflex is 
    not considered to be present, and the fuel storage pool water has a 
    high concentration of boron, a density decrease causes a positive 
    reactivity addition. The amount of soluble boron required to offset 
    this postulated accident was evaluated for the allowed storage 
    configurations. The amount of soluble boron necessary to mitigate 
    these accidents and ensure that the Keff will be 
    maintained less than or equal to 0.95 has been included in the fuel 
    storage pool boron concentration. Because adequate soluble boron 
    will be maintained in the pool water, the consequences of a loss of 
    normal cooling to the fuel storage pool will not be increased.
        Therefore, based on the conclusions of the above analysis, the 
    proposed changes will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The potential for criticality accidents in the fuel storage pool 
    are not new or different types of concerns. The potential 
    criticality accidents have been reanalyzed in the Criticality 
    Analysis report (Enclosure 5 [of the licensee's application]) to 
    demonstrate that the pool remains subcritical.
        Soluble boron has been maintained in the fuel storage pool water 
    since its initial operation. The possibility of a fuel storage pool 
    dilution is not affected by the proposed change to the Technical 
    Specifications. Therefore, the implementation of Technical 
    Specification controls for the soluble boron will not create the 
    possibility of a new or different kind of accidental pool dilution.
        With credit for soluble boron now a major factor in controlling 
    subcriticality, an evaluation of fuel storage pool dilution events 
    was completed. The results of the evaluation concluded that no 
    credible events would result in a reduction of the criticality 
    margin below the 5% margin recommended by the NRC. In addition, the 
    No Soluble Boron 95/95 criticality analysis assures that dilution to 
    0 ppm will not result in criticality.
        Proposed Technical Specifications 3.7.17, 3.7.18 and 4.3.1.1 
    which ensure the maintenance of the fuel storage pool boron 
    concentration and storage configuration, do not represent new 
    concepts. The actual boron concentration in the fuel storage pool 
    has been maintained at a higher value than the proposed limits for 
    the Unit 1 and 2 fuel storage pools for refueling purposes. The 
    criticality analysis (Enclosure 5 [of the licensee's application]) 
    determined that a boron concentration of 450 ppm (Unit 1) and 500 
    ppm (Unit 2) results in a Keff [less than or equal to] 
    0.95.
        There is no significant change in plant configuration, equipment 
    design, or usage of plant equipment. The safety analysis for 
    dilution accidents has been expanded; however, the criticality 
    analyses assure that the pool will remain subcritical with no credit 
    for soluble boron. Therefore, the proposed changes will not create 
    the possibility of a new or different kind of accident.
        3. The proposed change does not result in a significant 
    reduction in the margin of safety.
        Proposed Technical Specifications 3.7.17, 3.7.18, and 4.3.1.1 
    and the associated fuel storage pool boron concentration and storage 
    requirements will provide adequate margin to assure that the fuel 
    storage array will always remain subcritical by the 5% margin 
    recommended by the NRC. Those limits are based on the criticality 
    analysis (Enclosure 5 [of the licensee's application]) performed in 
    accordance with the Westinghouse fuel storage rack criticality 
    analysis methodology described in Reference 4 [of the licensee's 
    application].
        While the criticality analysis utilized credit for soluble 
    boron, the storage configurations have been defined using 
    Keff calculations to ensure that the spent fuel rack 
    Keff will be less than 1.0 with no soluble boron.
        Soluble boron credit is used to offset off-normal conditions 
    (such as a misplaced assembly) and to provide subcritical margin 
    such that the fuel storage pool Keff is maintained less 
    than or equal to 0.95.
        The combination of the No Soluble Boron 95/95 Keff 
    calculation which shows that the Keff will remain less 
    than 1.0 when flooded with unborated water and the unavailability of 
    the large volumes of water which are necessary to dilute the fuel 
    storage pool to a Keff of > 0.95, provide a level of 
    safety comparable to the conservative criticality analysis 
    methodology required by References 1, 2, and 3 [of the licensee's 
    application].
        Therefore, the proposed changes in this license amendment will 
    not result in a significant reduction in the plant's margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia.
        NRC Project Director: Herbert N. Berkow.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia
    
    Vogtle Electric Generating Plant, Units 1 and 2, Burke County, Georgia
    
    [Docket Nos. 50-424 and 50-425]
    
        Date of amendment request: September 4, 1997, as supplemented 
    November 20, 1997.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications (TS) to change the capacity of the 
    Vogtle Unit 1 spent fuel storage pool from 288 to 1476 assemblies, and 
    would revise the design features description to reflect the criticality 
    analyses and storage cell spacing. Specifically, the changes would be 
    as follows:
    
        1. Figure 3.7.18-1 would be replaced with a revised figure based 
    on the criticality analyses for the Unit 1 racks containing boral.
        2. The criticality information for Unit 2 would be placed 
    unchanged into Section 4.3.1.2, and Section 4.3.1.1. would be 
    revised to address Unit 1.
        3. Design Features Section 4.3.1.1.c would be revised to 
    indicate 600 ppm as the required amount of soluble born to maintain 
    Keff less than or equal to 0.95.
        4. Design Features Section 4.3.1.1.d would be revised to include 
    the reference Keff that is equivalent to the combination 
    of burnup and initial enrichment defined by Figure 3.7.18-1.
        5. Design Features Section 4.3.1.1.e would be revised to 
    indicate that fuel assemblies with up to 5 weight percent U-235 may 
    be stored in 3-out-of-4 checkerboard storage configurations; delete 
    Figure 4.3.1-1; eliminate the reference to 2-out-of-4 storage for 
    the Unit 1 pool and include the reference K acceptable for all cell 
    storage in the Unit 1 fuel storage racks.
        6. Design Features Section 4.3.1.1.f would be revised to include 
    the pitch of the Unit 1 fuel storage racks.
    
    [[Page 68318]]
    
        7. Design Features Section 4.3.3 would be revised to indicate 
    the Unit 1 fuel storage pool capacity of 1476 fuel assemblies.
        8. The titles on Figures 4.3.1-4, 4.3.1-6, and 4.3.1-7 would be 
    revised to reflect the elimination of 2-out-of-4 storage 
    configuration requirements for the Unit 1 fuel storage pool.
        Changes to the TS Bases are also proposed.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The analyses methodologies are the same as previously 
    approved for use by the NRC. The results of the analyses resulted in 
    fuel pool boron concentrations, and fuel assembly storage 
    limitations that are similar to those already submitted to the NRC. 
    The increased number of fuel assemblies will remain less than the 
    number previously accepted by the NRC for storage in VEGP [Vogtle 
    Electric Generating Plant] Unit 2, which has a similarly designed 
    and constructed facility, with the exception of the number of fuel 
    storage locations.
        Therefore, based on the conclusions of the above analysis, the 
    proposed changes will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The effects of accidents that could affect the fuel were 
    analyzed for the fuel storage racks, however the types of accidents 
    have not changed. The fuel to be stored in the Unit 1 pool is 
    expected to meet the all cell storage requirements. The racks will 
    be placed in the Unit 1 pool without lifting any loads over spent 
    fuel. After installation of the new racks, the Unit 1 pool will have 
    1476 storage locations which is well within the 2098 locations that 
    the pool and structure is capable of storing, based on its 
    similarity to the Unit 2 pool.
        Therefore, the proposed changes will not create the possibility 
    of a new or different kind of accident.
        3. The changes to the technical specifications are necessary to 
    incorporate the parameters resulting from the criticality analyses. 
    The criticality analyses were performed using methods and criteria 
    previously accepted by the NRC. The requirements are similar to the 
    previously submitted requirements. The margins of safety provided by 
    the previous technical specifications are not significantly affected 
    because the new racks are based on the same acceptance values. The 
    larger number of fuel assemblies to be stored in the Unit 1 pool 
    remains well within the capability of the pool.
        Therefore, the proposed changes in this license amendment will 
    not result in a significant reduction in the plant's margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia.
        NRC Project Director: Herbert N. Berkow.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia
    
    Vogtle Electric Generating Plant, Units 1 and 2, Burke County, Georgia
    
    [Docket Nos. 50-424 and 50-425]
    
        Date of amendment request: November 20, 1997.
        Description of amendment request: The proposed amendment would 
    change the Technical Specifications (TS) to provide for the following 
    with regard to the Reactor Trip System (RTS) and Engineered Safety 
    Feature Actuation System (ESFAS) instrumentation trip setpoints:
    
        1. The inequalities as they are applied to the Trip Setpoint 
    column of Tables 3.3.1-1 and 3.3.2-1 would be deleted, and the 
    column heading would be changed from ``Trip Setpoint'' to ``Nominal 
    Trip Setpoint.''
        2. A footnote would be added to the new ``Nominal Trip 
    Setpoint'' column of Tables 3.3.1-1 and 3.3.2-1 that would allow the 
    trip setpoints to be set more conservative than the nominal value as 
    necessary to respond to plant conditions.
        3. The Allowable Value for Table 3.3.1-1, Function 14.b, Turbine 
    Trip--Turbine Stop Valve Closure, would be revised from ``[greater 
    than or equal to] 96.7% open'' to ``[greater than or equal to] 90% 
    open.''
        4. Footnotes l and m of Table 3.3.1-1 would be revised to refer 
    to the ``Nominal Trip Setpoint'' and delete the inequalities applied 
    to the trip setpoints.
        5. A superscript ``(a)'' would be deleted from the heading of 
    the ``Trip Setpoint'' column on page 6 of 8 of Table 3.3.1-1.
        6. Notes 1 and 2 to Table 3.3.1-1, Overtemperature T 
    and Overpower T, respectively, would be revised to refer to 
    the ``Nominal Trip Setpoint.'' In addition, these notes will be 
    revised to delete the inequalities from the values for the constants 
    K1 through K6 (except for K5 
    [greater than or equal to] 0 for decreasing temperature and 
    K6 = 0 for T [less than or equal to] T''), and for T', 
    T'', and P'.
        7. The inequality applied to the ESFAS Allowable Value for Steam 
    Line Pressure--Low (Table 3.3.2-1, Function 1.e) would be changed 
    from ``[less than or equal to]'' to ``[greater than or equal to].''
        Associated changes to the TS Bases are also proposed.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the proposed change involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        No. The proposed changes affect only the presentation of the 
    trip set points for the RTS and ESFAS in the VEGP [Vogtle Electric 
    Generating Plant] Units 1 and 2 TS. The calibration of the channels 
    whose setpoints are specified in the TS will continue to be 
    performed in a manner consistent with the setpoint methodology 
    described in WCAP-11269 Rev. 1. There will be no adverse effect on 
    the ability of those channels to perform their safety functions as 
    assumed in the safety analyses. Since there will be no adverse 
    affect on the trip setpoints or the instrumentation associated with 
    those trip setpoints, there will be no increase in the probability 
    of any accident previously evaluated. Similarly, since the ability 
    of the instrumentation to perform its safety function is not 
    adversely affected, there will [be] no increase in the consequences 
    of any accident previously evaluated.
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        No. The proposed change affects only the presentation of trip 
    setpoint requirements in the TS. Plant operation will not be 
    changed, and the response of safety related equipment as assumed in 
    the accident analyses will not be adversely affected. Therefore, the 
    proposed change does not involve a new or different kind of accident 
    than any previously evaluated.
        3. Does the proposed change involve a significant reduction in a 
    margin of safety [?]
        No. As described above, the RTS and ESFAS instrumentation will 
    remain capable of performing its safety function as assumed in the 
    accident analyses. The treatment of trip setpoints as nominal values 
    is consistent with the methodology used to establish those 
    setpoints. As such, margin is not affected by the proposed change.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia.
        NRC Project Director: Herbert N. Berkow.
    
    [[Page 68319]]
    
    Vermont Yankee Nuclear Power Corporation
    
    [Docket No. 50-271]
    
    Vermont Yankee Nuclear Power Station, Windham County, Vermont
    
        Date of amendment request: October 10, 1997, as supplemented 
    October 31, 1997.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) to reflect the installation of 
    a generator no-load disconnect to facilitate use of the main step-up 
    transformer backfeed as the delayed access offsite power source. Also, 
    the amendment would revise existing limiting conditions for operation 
    and required action statements for operation with inoperable ac power 
    sources to be consistent with current guidance.
        Specifically, the changes proposed are: (1) TS Limiting Conditions 
    for Operation Section--Normal Operation, 3.10.A.4 (2) TS Limiting 
    Conditions for Operation Section--Operation with Inoperable Components, 
    3.10.B.3, (3) TS Surveillance Requirements--Normal Operation, 4.10.A.4, 
    (4) TS Surveillance Requirements--Operation with Inoperable Components, 
    Section 4.10.B.3, (5) Bases Section 3.10.A, (6) Bases Section 3.10.B, 
    (7) Bases Section 4.10.A, and (8) Bases Section 4.10.B
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        (1) The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment removes credit for the Vernon Tie, 
    Vermont Yankee's station blackout source of power, from the 
    Technical Specifications and reflects the installation of the 
    generator no load disconnect as part of the backfeed. Neither the 
    backfeed through the main transformers nor the Vernon Tie are 
    accident initiators; therefore, the change does not involve a 
    significant increase in the probability of an accident previously 
    evaluated. The change does not affect the capability, availability, 
    maintenance or operation of the Vernon Tie. Installation of the 
    generator no load disconnect switch is being implemented by a design 
    change in order to enhance plant safety by reducing time necessary 
    to establish the backfeed through the main transformer. A separate 
    10 CFR 50.59 evaluation is being prepared to document that the 
    modification does not create an unreviewed safety question.
        The proposed amendment also clarifies the allowable out of 
    service times, and required actions; and updates surveillance 
    requirements for the immediate and delayed access offsite power 
    sources. These changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    Modification of a technical specification out of service time and 
    required action cannot affect the probability or consequences of an 
    accident. Enhancing surveillance requirements to provide assurance 
    that the backfeed can be achieved when required and to provide 
    assurance that remaining power sources are available when an offsite 
    source is unavailable improves plant safety and does not increase 
    the probability or consequences of an accident.
        Therefore, the change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        (2) The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment removes the Vernon Tie, Vermont Yankee's 
    station blackout source of power, as a delayed access source from 
    the Technical Specifications and reflects the improvements to the 
    main transformer backfeed delayed access source because of 
    installation of the generator no load disconnect. Neither the 
    removal of the Vernon Tie from Technical Specifications nor the 
    improvements to the delayed access power source (backfeed) can 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        The proposed amendment also clarifies the allowed outage times, 
    and action statements; and updates surveillance requirements for the 
    immediate and delayed access offsite power sources. A clarification 
    of a technical specification out of service time and required action 
    cannot create a new or different kind of accident from any accident 
    previously evaluated. Enhancing surveillance requirements to provide 
    assurance that the backfeed can be achieved when required and to 
    provide assurance that remaining power sources are available when an 
    offsite source is unavailable improves plant safety and cannot 
    create a new or different kind of accident from any accident 
    previously evaluated.
        Therefore, this change would not create the possibility of a 
    different type of accident than previously evaluated.
        (3) The proposed amendment will not involve a significant 
    reduction in a margin of safety.
        The proposed amendment removes the Vernon Tie, Vermont Yankee's 
    station blackout source of power, as a delayed source of offsite 
    power from the Technical Specifications and reflects the 
    improvements to the main transformer backfeed delayed access source 
    because of installation of the generator no load disconnect. No 
    existing safety margins are adversely affected. The backfeed is 
    modified so that it may be established in sufficient time to 
    ``assure that specified acceptable fuel design limits and design 
    conditions of the reactor coolant pressure boundary are not 
    exceeded''. Vernon Tie will not be affected by the modification and 
    remain available as a station blackout source; thus this change does 
    not involve a significant reduction in the margin of safety.
        The proposed amendment also clarifies the allowed out of service 
    times, and required actions; and updates surveillance requirements 
    for the immediate and delayed access offsite power sources. A 
    clarification of a technical specification out of service time and 
    required action does not involve a significant reduction in the 
    margin of safety in the Technical Specifications. Enhancing 
    surveillance requirements to provide assurance that the backfeed can 
    be achieved when required and to provide assurance that remaining 
    power sources are available when an offsite source is unavailable 
    improves plant safety and does not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Project Director: Ronald Eaton, Acting Director.
    
    Vermont Yankee Nuclear Power Corporation
    
    [Docket No. 50-271]
    
    Vermont Yankee Nuclear Power Station, Windham County, Vermont
    
        Date of amendment request: November 20, 1997.
        Description of amendment request: The proposed amendment would 
    revise the existing requirements for the Auxiliary Electrical Power 
    Systems as identified in Technical Specifications (TSs) 3/4.10.A and TS 
    3.10.A.2.b. The specific changes are:
        (1) The requirements in TS 3.10.A.2.b. are revised to omit the 
    allowance for Spare Charger AB to substitute for either Charger A or B.
        (2) The Bases in TS 3.10.A. are revised to omit the statements that 
    justify Spare Charger AB to substitute for either Charger A or Charger 
    B.
        The proposed changes provide more limiting requirements for 
    operation with the standby battery charger in service.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
    
    [[Page 68320]]
    
        Neither batteries, nor their chargers, are considered to be an 
    initiator of any previously analyzed accident. Therefore, this 
    change will not significantly increase the probability of any 
    previously analyzed accident.
        At least one Battery System is required to be available to 
    mitigate the consequences of a Design Basis Accident. This change 
    removes an allowance which places the unit in a more vulnerable 
    condition through the unrestricted use of the spare battery charger. 
    Since this change limits such a condition, it maintains the 
    assumptions of the safety analysis, and therefore, will not 
    significantly increase the consequences of any previously analyzed 
    accident.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed change does not necessitate a physical alteration 
    of the plant (no new or different type of equipment will be 
    installed) nor is operation of the currently installed equipment 
    changed. The change will, however, limit a currently allowed 
    configuration with the spare charger and is more conservative. Thus, 
    this change will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety.
        The proposed change continues to provide the previous margin of 
    safety regarding the capability to withstand a single failure. At 
    least one Battery System will continue to be available to provide 
    the required safety function. The change will limit a currently 
    allowed configuration with the spare charger and is thus more 
    conservative. Therefore, this change will not significantly reduce a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Project Director: Ronald Eaton, Acting Director.
    
    Vermont Electric and Power Company
    
    [Docket Nos. 50-280 and 50-281]
    
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: November 5, 1997.
        Description of amendment request: The proposed change to Technical 
    Specifications 5.3 and 5.4 would reflect an increase in the maximum 
    permitted fuel enrichment to 4.3 weight percent U235 from 
    the current 4.1 weight percent U235. Fuel burnup limits and 
    reactor operating power level would remain unchanged.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Virginia Electric and Power Company has reviewed the Technical 
    Specifications changes for Surry Units 1 and 2 against the criteria 
    of 10 CFR 50.92. It has been concluded that use of fuel with the 
    slightly higher initial enrichment does not involve a significant 
    hazards consideration as defined in 10 CFR 50.92. An increase in the 
    maximum initial fuel enrichment from 4.1 to 4.3 weight percent 
    U235 will not:
        1. Involve a significant increase in the probability of 
    occurrence or the consequences of an accident previously evaluated. 
    The only accidents for which the probability of occurrence is 
    potentially affected by the fuel enrichment involve criticality 
    events during handling and storage. Analyses have demonstrated that 
    the K-effective will be low enough to ensure subcriticality during 
    both normal operation and under postulated accident conditions 
    during the handling and storage of both new and spent fuel. 
    Therefore, the probability of occurrence of criticality during fuel 
    handling or storage is not increased. Safety analyses of record are 
    based on inputs which bound the proposed increase in fuel 
    enrichment. Since no changes to the fuel burnup limits are 
    requested, the radiological consequences of previously evaluated 
    accident scenarios will not be increased. Therefore, neither the 
    probability of occurrence nor the consequences of any accident 
    previously evaluated is significantly increased.
        2. Create the possibility for a new or different type of 
    accident from any accident previously evaluated. Fuel with the 
    higher initial enrichment will meet all applicable design criteria 
    and will operate within existing Technical Specifications limits. 
    Adherence to these standards and criteria precludes new challenges 
    to components and systems that could introduce a new type of 
    accident. All design and performance criteria will continue to be 
    met. In addition, the use of a slightly higher initial fuel 
    enrichment does not involve any alteration to plant equipment or 
    procedures which would introduce any new or unique operational modes 
    or accident precursors. Therefore, the possibility for a new or 
    different kind of accident from any accident previously evaluated is 
    not created.
        3. Involve a significant reduction in the margin of safety. 
    Surry Units 1 and 2 will continue to operate in compliance with the 
    Technical Specifications, ensuring that the plants continue to 
    provide acceptable levels of protection for the health and safety of 
    the public. The Technical Specifications are based upon 
    assumption[s] made in the safety and accident analyses, including 
    those relating to the fuel enrichment and the design of the fuel 
    storage areas. Analyses have demonstrated that subcriticality will 
    be ensured during fuel storage and handling accident scenarios for 
    both new and spent fuel. Additionally, safety analyses of record for 
    core operation will remain applicable for Surry Unit 1 and 2 cores 
    which use fuel with the slightly higher U235 enrichment. 
    Therefore, the regulated margin of safety as defined in the Bases to 
    the Surry Technical Specifications is not reduced.
        Based on the preceding information, it has been determined that 
    the use of fuel with an initial enrichment of up to 4.3 weight 
    percent U235 satisfies the no significant hazards 
    consideration criteria of 10 CFR 50.92.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
        Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Swern Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: James E. Lyons.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these
    
    [[Page 68321]]
    
    amendments. If the Commission has prepared an environmental assessment 
    under the special circumstances provision in 10 CFR 51.12(b) and has 
    made a determination based on that assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company
    
    [Docket Nos. STN 50-454 and STN 50-455]
    
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois, Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: June 30, 1997, as supplemented 
    on September 25, 1997.
        Brief description of amendments: The amendments grant partial 
    credit for boron in the spent fuel pools to maintain the 
    subcriticality.
        Date of issuance: December 4, 1997.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 94, 94, 86 and 86.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: October 22, 1997 (62 FR 
    54868).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 4, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Duquesne Light Company, et al.
    
    [Docket Nos. 50-334 and 50-412]
    
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: March 14, 1997, as 
    supplemented. July 29, 1997, and August 13, 1997. The July 29, 1997, 
    and August 13, 1997, letters provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination or expand the amendment request beyond the scope of the 
    May 7, 1997, Federal Register notice.
        Brief description of amendments: These amendments relocate certain 
    administrative control Technical Specifications (TSs) from the Beaver 
    Valley Power Station, Unit Nos. 1 and 2 (BVPS-1 and BVPS-2), TSs to the 
    licensee's operational quality assurance program description, which is 
    presented in Section 17.2 of the BVPS-2 Updated Final Safety Analysis 
    Report (UFSAR). Section 17.2 of the BVPS-2 UFSAR contains the quality 
    assurance program description for both BVPS-1 and BVPS-2. The following 
    TSs are being relocated to the quality assurance program description.
    
    BVPS-2 TS 6.2.3 (Independent Safety Evaluation Group)
    BVPS-1 and BVPS-2 TS 6.5.1 (Onsite Safety Committee)
    BVPS-1 and BVPS-2 TS 6.5.2 (Offsite Review Committee)
    BVPS-1 and BVPS-2 TS 6.8.2 (Procedures, Review and)
    BVPS-1 and BVPS-2 TS 6.8.3 (Temporary Procedure Changes, Review and 
    Approval)
    BVPS-1 and BVPS-2 TS 6.10.1 (Records Retention, At least 5 Years)
    BVPS-1 and BVPS-2 TS 6.10.2 (Records Retention, Duration of Operating 
    License)
    
        Date of issuance: December 10, 1997.
        Effective date: Both units, as of date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 209 and 87.
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications, and Appendix C of the License.
        Date of initial notice in Federal Register: May 7, 1997 (62 FR 
    24986).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
    
    Entergy Operations, Inc.
    
    [Docket No. 50-382]
    
    Waterford Steam Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: July 17, 1996, as supplemented by 
    letters dated June 3, and July 7, 1997. Also, application dated April 
    11, 1997.
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specification (TS) 3.7.1.3 by increasing the minimum 
    required contained water volume in Condensate Storage Pool from 82 
    percent to 91 percent indicated level. In addition, this amendment 
    expands the applicability of TS 3.7.1.3 to include Mode 4 operational 
    requirements. The amendment also deletes Action (b) in TS 3.7.1.3 and 
    its associated surveillance requirement in Waterford 3 TSs.
        Date of issuance: December 18, 1997.
        Effective date: December 18, 1997, to be implemented within 60 
    days.
        Amendment No.: 137.
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14461), July 30, 1997 (62 FR 40849) and April 22, 1997 (62 FR 19624).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated December 18, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
    
    Florida Power Corporation, et al.
    
    [Docket No. 50-302]
    
    Crystal River Unit No. 3 Nuclear Generating Plant, Citrus County, 
    Florida
    
        Date of application for amendment: August 26, 1997.
        Brief description of amendment: The amendment involves a revision 
    to the design basis of the Emergency Diesel Generator (EDG) Air 
    Handling System at Crystal River 3 resulting from the EDG upgrade 
    modification which increased the 200-hour and 2000-hour service ratings 
    for each EDG.
        Date of issuance: December 12, 1997.
        Effective date: December 12, 1997.
        Amendment No.: 160.
        Facility Operating License No. DPR-31: Amendment revises the Final 
    Safety Analysis Report.
        Date of initial notice in Federal Register: September 24, 1997 (62 
    FR 50004).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated December 12, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal River, Florida 34428
    
    [[Page 68322]]
    
    Indiana Michigan Power Company
    
    [Docket Nos. 50-315 and 50-316]
    
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: September 19, 1997 
    (AEP:NRC:1278).
        Brief description of amendments: The amendments modify Technical 
    Specification 4.5.2.d.1 to delete the interlock that would close the 
    Residual Heat Removal (RHR) suction valves if the Reactor Coolant 
    System (RCS) pressure were to increase to 600 psig while retaining the 
    interlock that would prevent the suction valves from opening while the 
    RCS pressure is above the RHR system design pressure. This change 
    maintains the open interlock function and allows continued deactivation 
    of the isolation valves to assure RHR availability and provide low 
    temperature overpressure protection.
        Date of issuance: December 10, 1997.
        Effective date: December 10, 1997, with full implementation within 
    45 days.
        Amendment Nos.: 219 and 203.
        Facility Operating License Nos. DPR-58 and DPR-74: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 22, 1997 (62 FR 
    54861).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Pennsylvania Power and Light Company
    
    [Docket Nos. 50-387 and 50-388]
    
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: October 7, 1996, as 
    supplemented by letter dated May 9, 1997.
        Brief description of amendments: These amendments modify 
    Susquehanna Steam Electric Station, Units 1 and 2, Technical 
    Specifications Table 3.3.2-2 by revising the trip setpoints and 
    allowable values for secondary containment isolation radiation 
    monitors.
        Date of issuance: December 8, 1997.
        Effective date: December 8, 1997.
        Amendment Nos.: 170 and 143.
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 18, 1996 (61 
    FR 66716).
        The May 9, 1997, letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 8, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
    
    Pennsylvania Power and Light Company
    
    [Docket Nos. 50-387 and 50-388]
    
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: April 4, 1997, as supplemented 
    April 14, June 6, and September 2, 1997.
        Brief description of amendments: These amendments clarify the scope 
    of the surveillance requirements for response time testing of 
    instrumentation in the reactor protection system, isolation actuation 
    system, and emergency core cooling system in the Technical 
    Specifications for each unit (Sections 4.3.1.3, 4.3.2.3, and 4.3.3.3).
        Date of issuance: December 8, 1997.
        Effective date: December 8, 1997.
        Amendment Nos.: 171 and 144.
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 17, 1997 (62 FR 
    17885).
        The April 14, June 6, and September 2, 1997, letters provided 
    clarifying information that did not change the original proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 8, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
    
    Power Authority of the State of New York
    
    [Docket No. 50-333]
    
    James A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: December 14, 1995, as 
    supplemented September 26, 1997.
        Brief description of amendment: The amendment proposes to change 
    the James A. FitzPatrick Technical Specifications to incorporate the 
    inservice testing requirements of Section XI of the American Society of 
    Mechanical Engineers Boiler and Pressure Vessel Code.
        Date of issuance: December 2, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 241.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1635).
        The September 26, 1997, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated December 2, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Rochester Gas and Electric Corporation
    
    [Docket No. 50-244]
    
    R. E. Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: September 29, 1997, as 
    supplemented October 8, 1997.
        Brief description of amendment: The amendment revises the Ginna 
    Station Technical Specifications (TS) to allow referencing of revision 
    of the Ginna Station pressure and temperature limits report for the 
    reactor coolant system pressure and temperature limits and low 
    temperature overpressure protection limits. The amendment also corrects 
    a typographical error in the TSs.
        Date of issuance: December 9, 1997.
        Effective date: December 9, 1997.
        Amendment No.: 70.
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications.
    
    [[Page 68323]]
    
        Date of initial notice in Federal Register: November 5, 1997 (62 FR 
    59921).
        The September 29 and October 8, 1997, superseded in their entirety 
    the applications dated December 13, 1996, April 24, 1997, and June 3, 
    1997.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated December 9, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Southern California Edison Company, et al.
    
    [Docket Nos. 50-361 and 50-362]
    
    San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San Diego 
    County, California
    
        Date of application for amendments: December 22, 1995, as 
    supplemented by letter dated November 25, 1997.
        Brief description of amendments: These amendments revise License 
    Conditions 2.E and 2.G for the San Onofre Nuclear Generating Station 
    (SONGS), Units 2 and 3. The amendments delete the physical protection 
    program reporting requirement from License Condition 2.G, and clarify 
    in License Condition 2.E that not all documents composing the physical 
    protection program plans necessarily contain safeguards information.
        Date of issuance: December 16, 1997.
        Effective date: December 16, 1997.
        Amendment Nos.: Unit 2--138; Unit 3--130.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Facility Operating Licenses.
        Date of initial notice in Federal Register: November 5, 1997 (62 FR 
    59921). The November 25, 1997, letter provided additional clarifying 
    information and did not change the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated December 16, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Virginia Electric and Power Company, et al.
    
    [Docket Nos. 50-338 and 50-339]
    
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of application for amendments: May 14, 1997, as supplemented 
    October 15, 1997. The October 15, 1997, submittal provided clarifying 
    information only, and did not change the proposed no significant 
    hazards consideration determination.
        Brief description of amendments: The proposed action consists of 
    changes to the Technical Specifications (TS) revising Surveillance 
    Requirement 4.7.1.7.2.a for both units to clarify the testing and 
    inspection methodology of the turbine governor control valves. The 
    proposed changes also provide clarification in the TS Bases Section 3/4 
    7.1.7 for the Turbine Valve Freedom Testing of the turbine governor 
    control valves.
        Date of issuance: December 4, 1997.
        Effective date: December 4, 1997.
        Amendment Nos.: 207 and 188.
        Facility Operating License Nos. NPF-4 and NPF-7: Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: July 30, 1997 (62 FR 
    40860).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated December 4, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
        Dated at Rockville, Maryland, this 24th day of December 1997.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 97-33968 Filed 12-30-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
12/31/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-33968
Dates:
Immediately, to be implemented within 30 days.
Pages:
68303-68323 (21 pages)
PDF File:
97-33968.pdf