X96-21204. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 234 (Wednesday, December 4, 1996)]
    [Notices]
    [Pages 64381-64400]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-21204]
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from November 8, 1996, through November 21, 1996. 
    The last biweekly notice was published on November 19, 1996.
    
    NOTICE OF CONSIDERATION OF ISSUANCE OF AMENDMENTS TO FACILITY 
    OPERATING LICENSES, PROPOSED NO SIGNIFICANT HAZARDS CONSIDERATION 
    DETERMINATION, AND OPPORTUNITY FOR A HEARING
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By January 3, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible
    
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    effect of any order which may be entered in the proceeding on the 
    petitioner's interest. The petition should also identify the specific 
    aspect(s) of the subject matter of the proceeding as to which 
    petitioner wishes to intervene. Any person who has filed a petition for 
    leave to intervene or who has been admitted as a party may amend the 
    petition without requesting leave of the Board up to 15 days prior to 
    the first prehearing conference scheduled in the proceeding, but such 
    an amended petition must satisfy the specificity requirements described 
    above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: October 31, 1996
        Description of amendment request: The proposed change would revise 
    the maximum allowable water temperature as measured at the respective 
    intake structures from 95 deg.F to 94 deg.F and will increase the 
    minimum main reservoir level from 205.7 feet mean sea level to 215 feet 
    mean sea level in Technical Specification (TS) 3/4.7.5, Ultimate Heat 
    Sink.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Since the proposed change does not affect the operation of any 
    accident initiating systems, the probability of occurrence of an 
    accident previously evaluated will not increase. Also, none of the 
    proposed changes will cause plant systems to operate outside their 
    design limits or create the likelihood of a radioactive release. 
    Therefore, there would be no increase in the consequences of an 
    accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        No new component or system level interactions will be created by 
    the proposed change in ultimate heat sink level and temperature, and 
    no design limits will be exceeded. This change to [Technical] 
    Specification 3/4.7.5 is more conservative than the current 
    Specification limits and will serve only to restrict operation to a 
    higher reservoir level and lower temperature than was previously 
    allowed. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed amendment will establish a more conservative 
    minimum main reservoir level such that safety-related heat 
    exchangers served by Emergency Service Water will continue to remove 
    their design-basis accident heat loads. Establishing a higher 
    minimum reservoir level, combined with a more conservative reservoir 
    temperature assumption, will involve an increase in the margin of 
    safety. Also, the proposed change in maximum reservoir temperature 
    from 95 deg.F to 94 deg.F will not result in any reduction in the 
    margin of safety. A maximum pre-accident initial water temperature 
    of 94 deg.F is necessary to yield a post-accident (30-day) 
    calculated maximum inlet temperature less than or equal to the 
    design basis temperature of 95 deg.F. Therefore, the proposed change 
    does not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
    [[Page 64383]]
    
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Mark Reinhart, Acting
    
    Duke Power Company, Docket Nos. 50-413 and 50-414, Catawba Nuclear 
    Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: November 4, 1996
        Description of amendment request: The proposed amendments would 
    eliminate from the Technical Specifications, Section 4.7.13.1, the 
    ``during shutdown'' restriction pertaining to the 18-month Standby 
    Shutdown System (SSS) diesel generator inspection. Unlike Catawba 
    Nuclear Station, many nuclear plants do not have an SSS facility and 
    associated diesel generator. The requirements in the Technical 
    Specifications for the SSS diesel generator (shared between both units) 
    were patterned after similar requirements for the emergency diesel 
    generators. The current wording requires that both units be shut down 
    to perform the subject inspection.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ... The standard for determining that a Technical Specification 
    amendment request involves no significant hazards considerations 
    requires that operation of the facility in accordance with the 
    requested amendment will not:
        1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated; or
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or
        3) Involve a significant reduction in the margin of safety.
        Criterion 1
        The proposed amendment seeks to change the surveillance 
    requirements to allow the SSS DG [diesel generator] periodic 
    inspection with one or both units on line. The surveillance can be 
    safely completed as proposed without affecting unit operation. The 
    equipment would not be removed from service for a time that would 
    exceed the current Limiting Condition For Operation or the 
    appropriate action statement would be entered. The probability or 
    consequences of any accident previously evaluated will not be 
    significantly increased because the removal of the SSS DG from 
    service can be safely performed while one or both units are 
    operating.
        Criterion 2
        The proposed amendment change does not change any actual 
    surveillance requirements. The change simply allows the 18 month SSS 
    DG inspection to be performed at different unit conditions. The 
    performance of the surveillance with the units operating do not 
    require any new component configurations that would reduce the 
    ability of any equipment to mitigate an accident. The station is not 
    degraded beyond that which has been previously evaluated. Therefore 
    the proposed change does not create the possibility of a new or 
    different kind of accident.
        Criterion 3
        The allowed outage time for the SSS DG, as specified by the 
    Limiting Condition For Operation, defines the required margin of 
    safety for equipment operability. Removing the SSS DG from service 
    for periodic inspection and returning it to service within the 
    allowed outage time does not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    proposed amendments involve no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: October 30, 1996
        Description of amendment request: The proposed changes would (1) 
    completely rewrite Technical Specification (TS) 4.4.2 to incorporate a 
    prestressed concrete containment surveillance program that is 
    consistent with Regulatory Guide 1.35, (2) modify TS 3.6.7 by 
    establishing new Limiting Conditions for Operation and required actions 
    related to the structural integrity of the reactor buildings, (3) 
    incorporate an editorial change to TS 6.6.3 to reference the relocated 
    tendon surveillance reporting requirements, and (4) modify TS 3.6.7 
    Bases to describe the Reactor Building post-tensioning TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) Will the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No. The proposed amendment to Oconee Technical Specifications 
    involves the implementation of an enhanced surveillance program for 
    the reactor building prestressed concrete containment and the 
    assurance of appropriate station response to abnormal degradation of 
    the containment structure. The proposed change will move Oconee into 
    a surveillance program which is consistent with accepted industry 
    practice and a published NRC regulatory position. The adoption of 
    Regulatory Guide 1.35 as a basis for the periodic inspection of the 
    reactor building prestressed concrete containment and clearly 
    defined station response to any indication of structural 
    deterioration will assure acquisition of sufficient data to 
    demonstrate that structural integrity is maintained and, if 
    necessary, appropriate compensatory action(s) are taken. By assuring 
    that any adverse trends in the behavior of the prestressed concrete 
    containment are identified and acted upon in a timely manner, this 
    change does not increase the probability or consequences of an 
    accident previously evaluated.
        2) Will the change create the possibility of a new or different 
    kind of accident from any previously evaluated?
        No. The proposed amendment to Oconee Technical Specifications 
    involves the implementation of an enhanced surveillance program for 
    the reactor building prestressed concrete containment and the 
    assurance of appropriate station response to abnormal degradation of 
    the containment structure. By adopting Regulatory Guide 1.35 as a 
    basis for the surveillance inspection program for the reactor 
    building prestressed concrete containment and clearly defining 
    required station response to any indication of structural 
    deterioration, sufficient data will be obtained to demonstrate that 
    structural integrity is being maintained and that any adverse 
    behavioral trends are identified and acted upon in a timely manner. 
    Therefore, the proposed amendment does not create the possibility of 
    any type of accident: new, different or previously evaluated.
        3) Will the change involve a significant reduction in a margin 
    of safety?
        No. Margin of safety is associated with confidence in the 
    ability of the fission product barriers (i.e., fuel and fuel 
    cladding, Reactor Coolant System pressure boundary, and containment 
    structure) to limit the level of radiation dose to the public. The 
    proposed Technical Specifications amendment will move Oconee into a 
    surveillance program which is consistent with accepted industry 
    practice and a published regulatory position. By ensuring more 
    timely identification of, and response to, any adverse trend in the 
    behavior of the reactor building prestressed concrete containment, 
    continued maintenance of the structural integrity is enhanced. 
    Therefore, the ability of the containment structure to perform the 
    intended function of protecting the public
    
    [[Page 64384]]
    
    from radiation dose is further assured, and no reduction in any 
    existing margin of safety will occur.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: September 9, 1996
        Description of amendment request: The proposed amendment would 
    modify the design features section (Section 5.0) of the Technical 
    Specifications (TSs) to make the design features section consistent 
    with the four criteria specified in the Commission's Policy Statement 
    on TSs (58 FR 39132) and with the guidance provided in the NRC's 
    Standard Technical Specifications, Westinghouse Plants (NUREG-1431, 
    Revision 1).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change reduces the content of the technical 
    specification (TS) design feature section consistent with the 
    Improved Standard Technical Specifications (ISTS) of NUREG-1431. The 
    information that has been removed is also contained in the UFSAR 
    [Updated Final Safety Analysis Report] or offsite dose calculation 
    manual (ODCM); therefore, duplication of the information is 
    eliminated to improve the use of the TS. Because the information 
    removed from the TS is maintained in the UFSAR or ODCM where changes 
    are controlled in accordance with regulatory requirements, there is 
    no reduction in commitment and adequate control is provided. 
    Elimination of information from the design feature section of the TS 
    which duplicates information in the UFSAR enhances the usability of 
    the TS without reducing commitments. These changes clarify and 
    improve the understanding and readability of the TS. Since the 
    requirements remain the same, these changes only affect the method 
    of presentation and would not affect possible initiating events for 
    accidents previously evaluated or any system functional requirement. 
    Therefore, the proposed changes would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The relocation of existing requirements, the elimination of 
    requirements which duplicate existing information, and making 
    administrative improvements are all changes that are administrative 
    in nature. The proposed changes will not affect any plant system or 
    structure, not [nor] will they affect any system functional or 
    operability requirements. Consequently, no new failure modes are 
    introduced as a result of the proposed changes. The proposed changes 
    are consistent with the ISTS, for the most part, as plant-specific 
    information is included in this section. Therefore, the proposed 
    change will not create the possibility of a new or different type of 
    accident from any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes are administrative in nature in that no 
    change to the design features of the facility are being made. The 
    design features section is being reformatted to be consistent, for 
    the most part, with the ISTS. The proposed changes do not affect the 
    UFSAR design bases, accident assumptions, or technical specification 
    bases. In addition, the proposed changes do not affect release 
    limits, monitoring equipment or practices. Therefore, the proposed 
    change will not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: October 24, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications to remove accelerated testing 
    requirements for the standby diesel generators. The changes implement 
    the provisions of Generic Letter (GL) 94-01, ``Removal of Accelerated 
    Testing and Special Reporting Requirements For Diesel Generators'', 
    dated May 31, 1994.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. This request does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        This change will provide flexibility to structure the standby 
    diesel generator maintenance program based on the risk significance 
    of the structures, systems, and components that are within the scope 
    of the Maintenance Rule. The removal of the diesel generator 
    accelerated testing is acceptable as the maintenance rule applies 
    site and system specific performance criteria to monitor diesel 
    generator performance. This criteria includes a running availability 
    and reliability goal as well as specific goals to monitor 
    maintenance preventable functional failures. The performance 
    criteria for the diesel generator reliability and unavailability 
    established by the maintenance rule and the causal determinations 
    and corrective actions required for maintenance preventable 
    functional failures are considered to be an acceptable method for 
    monitoring diesel generator performance.
        The proposed change has no effect on the probability of the 
    initiation of an accident, because the emergency diesel generators 
    do not serve as the initiator of any event. Additionally, as diesel 
    generator performance will continue to be assured by the maintenance 
    rule, the proposed changes do not affect the ability to mitigate the 
    consequences of an accident previously evaluated. The changes do not 
    impact the diesel's design sources, operating characteristics, 
    system functions, or system interrelationships. The failure 
    mechanisms for the accidents previously analyzed are not affected 
    and no additional failure modes are created that could cause an 
    accident that has been previously evaluated. Since the diesel 
    generator performance and reliability will continue to be assured by 
    the maintenance rule, the proposed changes cannot involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. This request does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        This proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed changes does not 
    affect any of the parameters or conditions that could contribute to 
    the initiation of any accidents. The proposed changes only affect 
    the methods used to monitor and assure diesel generator performance. 
    The performance criteria for both the diesel generator reliability 
    and unavailability established by the maintenance rule, and the
    
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    casual determinations and corrective actions required for 
    maintenance preventable functional failures, is considered by GL 94-
    01 to be an acceptable method for monitoring diesel generator 
    performance.
        No [system, structure, or component] SSC, method of operating, 
    or system interface is altered by this change. The changes do not 
    impact the diesel's design sources, operating characteristics, 
    system functions, or system interrelationships. The failure 
    mechanisms for the accidents are not affected, and no additional 
    failure modes are created. Because the diesel generator performance 
    and reliability will continue to be assured by the maintenance rule, 
    the proposed changes cannot create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The request does not involve a significant reduction in a 
    margin to safety.
        The proposed changes only affect the methods used to monitor and 
    assure diesel generator performance and reliability. The performance 
    criteria for both the diesel generator reliability and 
    unavailability established by the maintenance rule, and the casual 
    determinations and corrective actions required for maintenance 
    preventable functional failures, is considered by GL 94-01 to be an 
    acceptable method for monitoring diesel generator performance. No 
    margin to safety as defined in the basis for any technical 
    specification is impacted by these changes. This change does not 
    impact any uncertainty in the design, construction, or operation of 
    any SSC. Diesel generator response to accident initiators is 
    unchanged. No SSC, method of operating, or system interface is 
    altered by this change. The changes do not impact the diesel's 
    design sources, operating characteristics, system functions, or 
    system interrelationships. Because the diesel generator performance 
    and reliability will continue to be assured by the maintenance rule, 
    the proposed changes cannot involve a significant reduction in the 
    margin to safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 6, 1996
        Description of amendment request: The proposed amendment would 
    revise the River Bend Station (RBS) Fire Hazards Analysis Report and 
    Safety Analysis Report to allow a deviation from 10 CFR Part 50, 
    Appendix R, Section III.G.2.c with respect to the requirement for an 
    area wide automatic fire suppression system in Fire Area C-16. The 
    deviation would allow a 1-hour barrier to separate redundant trains of 
    post fire safe shutdown equipment within the fire area and partial 
    sprays on the protected train.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The request does not involve an increase in the probability 
    or consequences of an accident previously evaluated.
        The event of concern is a fire in Fire Area C-16. The low fire 
    loading and minimal concentration of exposed combustible material in 
    Fire Area C-16 would limit fire spread. However, for this scenario, 
    all unprotected equipment in Fire Area C-16 will be assumed lost. 
    Fire Area C-16 contains cables for both Division I and Division II 
    components required for post fire safe shutdown. The loss of both 
    divisions of cables could preclude the ability of the plant to 
    achieve post fire safe shutdown. Protection of the required Division 
    II cables in a 1-hour fire barrier in conjunction with a partial 
    area, automatic suppression system installed above and below the 
    protected trays will ensure that post fire safe shutdown can be 
    achieved.
        In summary, the probability of a fire occurring in Fire Area C-
    16 is not affected. However, if a fire were to occur in Fire Area C-
    16 which caused the loss of Division I powered components, Division 
    II powered components, by virtue of the 1-hour fire barrier and 
    partial area, automatic suppression system, would remain available. 
    The low fire loading and minimal concentration of exposed 
    combustible material in Fire Area C-16 would limit fire spread. The 
    proposed fire protection scheme provides a level of protection 
    commensurate with the original design. Therefore, this request does 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The request does not create the possibility of occurrence of 
    a new or different kind of accident from any accident previously 
    evaluated.
        Fire Area C-16 will be protected by a partial area, automatic 
    suppression system installed above and below the protected cable 
    trays. Fire suppression systems are generally used to limit fire 
    spread, once the heat of the fire opens thermally sensitive 
    sprinklers. The low fire loading and minimal concentration of 
    exposed combustible material in Fire Area C-16 would aid in limiting 
    fire spread, and would also limit the severity of any plausible 
    fire. The previous analysis assumed all Division I components and 
    cables in the area would be lost, and that the installed fire 
    barrier would adequately protect the Division II cables routed 
    through C-16. The required Division II cables will be enclosed in a 
    1-hour fire barrier with a partial area, automatic suppression 
    system. These features provide a level of protection commensurate 
    with that of the previous design. In addition, the total combustible 
    loading in the area results in a maximum theoretical worst case fire 
    duration of less than 1-hour.
        In summary, if a fire were to occur in Fire Area C-16 which 
    caused the loss of Division I powered components, post fire safe 
    shutdown could still be achieved using Division II. Therefore, this 
    request does not create the possibility of occurrence of a new or 
    different kind of accident from any accident previously evaluated.
        3. The request does not involve a significant reduction in a 
    margin of safety.
        In this case, the margin of safety is implicit rather than being 
    explicitly expressed as a numerical value. An implicit margin of 
    safety involves conditions for NRC acceptance. Since the RBS 
    Technical Specification Bases do not specifically address a margin 
    of safety for fire protection, the SAR [Safety Analysis Report], the 
    NRC's Safety Evaluation Report (SER), and appropriate other 
    licensing basis documents were reviewed to determine if the proposed 
    change would result in a reduction in a margin of safety. As stated, 
    in part, in Attachment 4 to NPF-47 [Facility Operating License; NPF-
    47]:
        EOI [Entergy Operations, Inc.] shall implement and maintain in 
    effect all provisions of the approved fire protection program as 
    described in the Final Safety Analysis Report for the facility 
    through Amendment 22 and as approved in the SER dated May 1984 and 
    Supplement 3 dated August 1985 subject to provisions 2 and 3 ....
        As discussed in the Reason for Request, SSER [Supplemental 
    Safety Evaluation Report] 3 dated August 1985 states, in part:
        On the basis of its evaluation the staff finds that the 
    applicant's fire protection program with approved deviations is in 
    conformance with the guidelines of BTP CMEB [branch technical 
    position, Chemical Materials and Engineering Branch] 9.5-1, 
    [S]sections III.G, III.J, and III.O of Appendix R to 10 CFR [Part] 
    50, and GDC [General Design Criteria] 3, and is, therefore, 
    acceptable.
        Thus, the margin of safety in this case can be defined as 
    conformance with the specified fire protection guidelines.
        10 CFR [Part] 50, Appendix R, Section III.G.2, requires, in 
    part, that redundant trains of post fire safe shutdown equipment 
    located in the same fire area be separated by a 1-hour fire barrier 
    and, in addition, that fire detection and an automatic fire 
    suppression system be installed in the are under consideration. 
    Since Fire Area C-16 will have a partial area, automatic suppression 
    system, this fire area would deviate from the requirements of 10 CFR 
    [Part] 50, Appendix R, Section III.G.2.c. However, as discussed 
    previously, the installed partial area, automatic suppression 
    system, the low fire loading and minimal amount of exposed 
    combustibles compensate for the lack of a total, area wide, 
    automatic fire suppression
    
    [[Page 64386]]
    
    system. There is no adverse impact on the ability to achieve and 
    maintain post fire safe shutdown. Therefore, this request does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant Units 1 and 2, St. Lucie County, Florida
    
        Dates of amendment requests: October 28, 1996 (Two letters)
        Description of amendment request: The licensee proposed to change 
    the St. Lucie Units 1 and 2 Technical Specifications (TS) to implement 
    10 CFR 50, Appendix J, Option B, for containment leakage testing by 
    referring to Regulatory Guide 1.163, ``Performance-Based Containment 
    Leakage-Test Program.'' Changes include relocating the details for 
    containment testing to the ``containment leakage rate testing program'' 
    and adding the requirements of the containment leakage rate testing 
    program to TS 6.8.4, which describes facility programs. Changes are 
    also proposed to remove Tables 3.6-1, ``Containment Leakage Paths,'' 
    and 3.6-2, ``Containment Isolation Valves'' from TS and relocate the 
    information to plant procedures.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    due to the following reasons:
        a)These proposed changes are all consistent with NRC 
    requirements and guidance for implementation of 10 CFR 50, Appendix 
    J, Option B, except for the use of Bechtel Topical Report BN-TOP-1 
    for type A testing. BN-TOP-1 has been previously approved for use in 
    accordance with 10 CFR 50 appendix J.
        b) Based on industry and NRC evaluations performed in support of 
    developing Option B, these changes potentially result in a minor 
    increase in the consequences of an accident previously evaluated due 
    to the increased testing intervals. However, the proposed changes do 
    not result in an increase in the core damage frequency since the 
    containment system is used for mitigation purposes only.
        c) These changes are expected to result in increased attention 
    to components with poor leakage test history as part of the 
    performance-based nature of Option B, such that the marginally 
    increased consequences from the expanded testing intervals may be 
    further reduced or negated.
        Therefore, these changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.(2) Operation of the facility in accordance with the 
    proposed amendments would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The use of the modified specifications can not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated since the proposed amendments will not change 
    the physical plant or the modes of plant operation defined in the 
    facility operating license. No new failure mode is introduced due to 
    the implementation of a performance-based program for containment 
    leakage rate testing, since the proposed changes do not involve the 
    addition or modification of equipment, nor do they alter the design 
    or operation of affected plant systems, structures, or 
    components.(3) Operation of the facility in accordance with the 
    proposed amendments would not involve a significant reduction in a 
    margin of safety.
        The operating limits and functional capabilities of the affected 
    systems, structures, and components are basically unchanged by the 
    proposed amendments. The increase in intervals between leak-test 
    surveillances will not significantly reduce the margin of safety as 
    shown by findings in NUREG 1493, ``Performance-Based Containment 
    Leak-Test Program'', which was based on implementation of the 
    performance-based testing of Option B.
        Therefore these changes do not involve a significant reduction 
    in the margin of safety.The NRC staff has reviewed the licensee's 
    analysis and, based on thisreview, it appears that the three 
    standards of 50.92(c) are satisfied.Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: M. S. Ross, Attorney, Florida Power & Light, 
    11770 US Highway 1, North Palm Beach, Fl 33408
        NRC Project Director: Frederick J. Hebdon
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389,St. Lucie Plant Units 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: October 30, 1996
        Description of amendment request: The proposed amendments will 
    revise Technical Specification (TS) 3/4.9.10, ``Refueling Operations, 
    Water Level-Reactor Vessel.'' The Limiting Condition for Operation 
    (LCO) specified for the minimum allowed refueling water level is not 
    altered, but the Applicability, Action, and Surveillance Requirements 
    are changed to remove inconsistencies with the definition of Core 
    Alterations, and to achieve consistency with the generic Standard 
    Technical Specifications for Combustion Engineering Plants (NUREG-
    1432). An editorial change is proposed for TS 3/4.9.9, ``Refueling 
    Operations, Containment Isolation System,'' and, for St. Lucie Unit 1, 
    the LCO is modified to conform with other related refueling 
    specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Certain evolutions performed with the UGS [upper guide 
    structure] in place are not Core Alterations, and the revised LCO 3/
    4.9.10 will allow these activities to be performed at water levels 
    other than prescribed by the existing LCO. Since these activities 
    are performed with the UGS in place, the probability that a fuel 
    handling accident would occur is not impacted by the proposed 
    changes. The minimum water level required for Core Alterations and 
    movement of irradiated fuel in containment is not altered by the 
    proposed changes, nor are any assumptions or conditions changed that 
    were used as inputs to the evaluation of fuel handling accident 
    consequences. The changes to Specification 3/4.9.9 are 
    administrative in nature and resolve an inconsistency between the 
    operability requirements for the containment isolation system and 
    the containment penetrations that the system would isolate at PSL1 
    [Plant St. Lucie 1]. Therefore, operation of either facility in 
    accordance with its proposed amendment would not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different
    
    [[Page 64387]]
    
    kind of accident from any accident previously evaluated.
        The proposed changes are administrative in nature, in that the 
    changes do not involve the addition or modification of equipment nor 
    do they alter the design of plant systems. New failure modes are not 
    introduced, and the physical plant or the modes of plant operation 
    defined in the Facility License are not altered. Therefore, 
    operation of either facility in accordance with its proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The safety margin associated with a fuel handling accident is 
    determined, in part, by the minimum refueling water level allowed 
    for conducting Core Alterations and movement of irradiated fuel in 
    containment. The minimum water level required by LCO 3/4.9.10, or 
    other factors considered as inputs to the safety analysis, is not 
    changed by the proposed amendments. The revised applicability 
    requirements for LCO 3/4.9.9 at PSL1 will allow the containment 
    isolation system to be inoperable only during those Mode 6 
    conditions where Core Alterations or irradiated fuel movements 
    within containment are not in progress, or each required containment 
    penetration is otherwise closed. Therefore, operation of either 
    facility in accordance with its proposed amendment would not involve 
    a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendmentrequest involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: M. S. Ross, Attorney, Florida Power & Light, 
    11770 US Highway 1, North Palm Beach, Fl 33408
        NRC Project Director: Frederick J. Hebdon
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: October 23, 1996, as supplemented by 
    letter dated November 6, 1996.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 3.4.6.1, regarding reactor coolant 
    system leakage detection instrumentation, to adopt the requirements 
    found in NUREG-1431, ``Standard Technical Specifications Westinghouse 
    Plants,'' for the reactor coolant system leakage detection 
    instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involved a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change reduces the number of containment 
    atmospheric radioactivity channels which must be OPERABLE when 
    operating in MODES 1, 2, 3, and 4 from two to one. This change does 
    not significantly increase the probability or consequences of a 
    previously evaluated accident since the plant will continue to have 
    diverse and independent means of detecting significant changes in 
    the amount of leakage from the RCS [reactor coolant system]; the 
    normal sump level and flow monitoring system, at least one of the 
    two containment atmospheric radiation monitors, and the periodic 
    precision RCS water inventory balance required by Technical 
    Specification surveillance requirement 4.4.6.2.1.c. In addition, STP 
    [South Texas Project] design includes advanced trending displays 
    which can assist in detecting leakage based on changes in the volume 
    control tank or pressurizer level. Other instruments, which are not 
    listed in the Technical Specification related to leakage, but which 
    can provide indication of leakage, are the containment pressure, 
    temperature and humidity indicators. Good operating practice and 
    commercial risk associated with long term inoperability of both 
    monitors assures that an inoperable containment atmospheric 
    radiation monitor will be promptly returned to service.
        The proposed change also revises the limitation on continued 
    operation with both containment atmospheric radiation monitors 
    inoperable from 72 hours to 30 days. This change is based on the 
    continued availability of diverse and redundant instrumentation 
    discussed above to detect and indicate RCS leakage.
        The Actions required as a result of this change include analysis 
    of a containment atmospheric grab sample or performance of a 
    precision RCS water inventory balance in accordance with 
    surveillance requirement 4.4.6.2.1.c. The containment normal sump 
    level flow monitoring system will also promptly identify changes in 
    RCS leakage. Other installed instrumentation, such as containment 
    pressure, temperature, and humidity, will provide indications of 
    significant increases in leakage. Slower increases will be detected 
    by the daily inventory balance or the daily grab samples analysis, 
    and the three day inventory balance.
        Inoperability of the on-line automatic containment normal sump 
    level and flow monitoring system can be compensated for by the 
    performance of a daily manual calculation, a precision RCS inventory 
    balance as described in surveillance requirement 4.4.6.2.1.c, or the 
    other available indications of increases in leakage such as the 
    containment atmospheric radiation monitoring instruments and 
    installed containment temperature, pressure and humidity 
    instrumentation. The STP control room design also incorporates 
    features which allow rapid detection of unexpected changes in the 
    volume control tank and pressurizer level through available 
    instrument trend displays. The combination of the compensatory 
    measures, diverse and separate channels, and non-TS [non-technical 
    specification] required instrumentation provides a sufficient level 
    of detection to assure prompt identification and quantification of 
    leakage with an inoperable containment normal sump level and flow 
    monitoring system. The allowable outage time of 30 days provides 
    assurance the normal containment sump level and flow monitoring 
    system will be returned to service in a reasonable amount of time.
        Based on the continued availability of adequate and redundant 
    instrumentation to detect changes in RCS leakage rate, this change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not require the installation of any new 
    or different kind of equipment. Nor does the change involve any 
    significant new or different MODE of operation of the plant. The 
    proposed change reduces the number of required containment 
    atmospheric radiation monitors, and provides a 30 day allowed outage 
    time for either the containment atmosphere radioactivity monitor or 
    the containment normal sump level and flow monitoring system. 
    Therefore, this change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        In addition, as described above, the proposed change does not 
    significantly reduce a margin of safety. Small changes in RCS leak 
    rates are typically detected over a relatively long period of time. 
    Diverse instrumentation continues to be available to plant operators 
    which will assist in early detection of any change. The STP design 
    provides additional non-Technical Specification human factors which 
    assist in assuring any changes in leakage will be quickly detected.
        The proposed change extends the amount of time that the 
    containment atmospheric radiation monitors may be inoperable. The 
    extension is based on the continued availability of equipment which 
    provides a level of detection capability adequate to detect 
    increases in RCS leakage and which continues to be diverse and 
    independent. This protection is afforded by the continued 
    OPERABILITY of the containment normal sump level and flow monitoring 
    system, the daily performance of a precision RCS
    
    [[Page 64388]]
    
    inventory balance as described by surveillance requirement 
    4.4.6.2.1.c or the daily analysis of containment atmospheric grab 
    samples, and other instrumentation such as pressure, temperature and 
    humidity indicators.
        The combination of the compensatory measures, diverse and 
    separate channels, and non-TS required instrumentation provides a 
    sufficient level of detection to assure prompt identification and 
    quantification of leakage with an inoperable containment normal sump 
    level and flow monitoring system. Additionally, the compensatory 
    measure of performing either a daily manual calculation or precision 
    RCS inventory balance, provides assurance that the level of safety 
    is maintained when the containment normal sump level and flow 
    monitoring system is inoperable. The allowable outage time of 30 
    days provides assurance the normal containment sump level and flow 
    monitoring system will be returned to service in a reasonable amount 
    of time.
        Based on the compensatory actions and available installed 
    equipment, the proposed changes do not represent a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869
        NRC Project Director: William D. Beckner
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: August 15, 1996
        Description of amendment requests: The proposed amendments would 
    revise the Containment Cooling Systems Limiting Conditions for 
    Operation Technical Specifications to bring them into conformance with 
    recently completed system analyses by no longer permitting both 
    containment spray pumps to be inoperable at the same time.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Operation of the Prairie Island plant in accordance with the 
    proposed changes does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    None of the proposed changes involve a physical modification to the 
    plant.
        These changes will require operability of at least one 
    containment spray pump at all times and reduces the spray additive 
    tank allowable outage time from 72 hours to 24 hours. Both of these 
    changes are more conservative and safer than currently required in 
    the Prairie Island Technical Specifications. These proposed changes 
    do allow one containment fan cooler train out of service for 7 days 
    instead of 72 hours as allowed by current Technical Specifications. 
    Recent plant analyses confirm that one containment fan cooler train 
    with one containment spray train is sufficient to meet the system 
    design bases. Since the probability of an accident occurring is low 
    while one containment fan cooler train is out of service, the 
    probability and consequences of an accident are not significantly 
    increased.
        In total these changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    because the proposed changes, in themselves, do not introduce a new 
    mode of plant operation, surveillance requirement or involve a 
    physical modification to the plant.
        The proposed changes do require more restrictive, safer 
    containment spray train operability. The proposed changes also allow 
    one containment fan cooler train to be out of service for 7 days 
    instead of 72 hours as allowed by the current Technical 
    Specifications. However, this change does not create the possibility 
    of a new kind of accident.
        The proposed changes do no alter the design, function, or 
    operation of any plant components and therefore, no new accident 
    scenarios are created.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be created 
    by these amendments.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety. This License Amendment Request 
    require[s] one containment spray train to be operable at all times 
    which is more restrictive than current Technical Specifications and 
    thus the margin of safety is not reduced.
        This License Amendment Request will also allow one containment 
    fan cooler train to be out of service for 7 days instead of 72 hours 
    as allowed by the current Technical Specifications. Since the 
    remaining containment cooling components can mitigate an accident 
    and the probability of a design basis accident are low during this 
    time, this change does not significantly reduce the plant margin of 
    safety.
        Therefore, a significant reduction in the margin of safety would 
    not be involved with these amendments.
        Based on the evaluation described above, and pursuant to 10 CFR 
    Part 50, Section 50.91, Northern States Power Company has determined 
    that operation [of] the Prairie Island Nuclear Generating Plant in 
    accordance with the proposed license amendment request does not 
    involve any significant hazards considerations as defined by Nuclear 
    Regulatory Commission regulations in 10 CFR Part 50, Section 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: September 24, 1996, as supplemented 
    October 17, 1996.
        Description of amendment requests: The proposed amendments would 
    revise the Technical Specifications (TS) for the Prairie Island Nuclear 
    Generating Plant to allow use of an alternate steam generator tube 
    repair criteria (elevated F-star or EF*) in the tubesheet region when 
    used with the repair method of additional roll expansion. The 
    amendments incorporate revised acceptance criteria for tubes with 
    degradation in the tubesheet region and enable the licensee to avoid 
    unnecessary plugging and sleeving of steam generator tubes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The supporting technical and safety evaluations of the subject 
    criterion
    
    [[Page 64389]]
    
    demonstrate that the presence of the tubesheet will enhance the tube 
    integrity in the region of the hardroll by precluding tube 
    deformation beyond its initial expanded outside diameter. The 
    resistance to both tube rupture and tube collapse is strengthened by 
    the presence of the tubesheet in that region. The results of 
    hardrolling of the tube into the tubesheet is an interference fit 
    between the tube and the tubesheet. Tube rupture cannot occur 
    because the contact between the tube and tubesheet does not permit 
    sufficient movement of tube material. The radial preload developed 
    by the rolling process will secure a postulated separated tube end 
    within the tubesheet during all plant conditions. In a similar 
    manner, the tubesheet does not permit sufficient movement of tube 
    material to permit buckling collapse of the tube during postulated 
    LOCA [loss-of-coolant accident] loadings.
        The EF* length of roll expansion is sufficient to preclude tube 
    pullout from tube degradation located below the EF* distance, 
    regardless of the extent of the tube degradation. The existing 
    Technical Specification leakage rate requirements and accident 
    analysis assumptions remain unchanged in the unlikely event that 
    significant leakage from this region does occur. As noted above, 
    tube rupture and pullout is not expected for tubes using the EF* 
    criterion. Any leakage out of the tube from within the tubesheet at 
    any elevation in the tubesheet is fully bounded by the existing 
    steam generator tube rupture analysis included in the Prairie Island 
    Plant USAR [updated safety analysis report]. For plants with partial 
    depth roll expansion like Prairie Island, a postulated tube 
    separation within the tube near the top of the roll expansion (with 
    subsequent limited tube axial displacement) would not be expected to 
    result in coolant release rates equal to those assumed in the USAR 
    for a steam generator tube rupture event due to the limited gap 
    between the tube and tubesheet. The proposed plugging criterion does 
    not adversely impact any other previously evaluated design basis 
    accident.
        Leakage testing of roll expanded tubes indicates that for roll 
    lengths approximately equal to the EF* distance, any postulated 
    faulted condition primary to secondary leakage from EF* tubes would 
    be insignificant.
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        Implementation of the proposed EF* criterion does not introduce 
    any significant changes to the plant design basis. Use of the 
    criterion does not provide a mechanism to initiate an accident 
    outside of the region of the expanded portion of the tube. Any 
    hypothetical accident as a result of any tube degradation in the 
    expanded portion of the tube would be bounded by the existing tube 
    rupture accident analysis. Tube bundle structural integrity will be 
    maintained. Tube bundle leaktightness will be maintained such that 
    any postulated accident leakage from EF* tubes will be negligible 
    with regard to offsite doses.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety.
        The use of the EF* criterion has been demonstrated to maintain 
    the integrity of the tube bundle commensurate with the requirements 
    of Reg Guide 1.121 [Bases for Plugging Degraded PWR Steam 
    Generator Tubes] (intended for indications in the free 
    span of tubes) and the primary to secondary pressure boundary under 
    normal and postulated accident conditions. Acceptable tube 
    degradation for the EF* criterion is any degradation indication in 
    the tubesheet region, more than the EF* distance below the bottom of 
    the transition between the roll expansion and the unexpanded tube. 
    The safety factors used in the verification of the strength of the 
    degraded tube are consistent with the safety factors in the ASME 
    [American Society of Mechanical Engineers] Boiler and Pressure 
    Vessel Code used in steam generator design. The EF* distance has 
    been verified by testing to be greater than the length of roll 
    expansion required to preclude both tube pullout and significant 
    leakage during normal and postulated accident conditions. Resistance 
    to tube pullout is based upon the primary to secondary pressure 
    differential as it acts on the surface area of the tube, which 
    includes the tube wall cross-section, in addition to the inner 
    diameter based area of the tube. The leak testing acceptance 
    criteria are based on the primary to secondary leakage limit in the 
    Technical Specifications and the leakage assumptions used in the 
    USAR accident analyses.
        Implementation of the tubesheet plugging criterion will decrease 
    the number of tubes which must be taken out of service with tube 
    plugs or repaired with sleeves. Both plugs and sleeves reduce the 
    RCS (reactor coolant system) flow margin; thus, implementation of 
    the EF* criterion will maintain the margin of flow that would 
    otherwise be reduced in the event of increased plugging or sleeving.
        Based on the above, it is concluded that the proposed change 
    does not result in a significant reduction in margin with respect to 
    plant safety as defined in the USAR or the Technical Specification 
    Bases.
        Based on the evaluation described above, and pursuant to 10 CFR 
    Part 50, Section 50.91, Northern States Power Company has determined 
    that operation of the Prairie Island Nuclear Generating Plant in 
    accordance with the proposed license amendment request does not 
    involve any significant hazards considerations as defined by NRC 
    regulations in 10 CFR Part 50, Section 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: June 10, 1996, as supplemented July 25, 
    1996
        Description of amendment request: The proposed amendment would 
    change the differential temperature Technical Specification Allowable 
    Values and Trip Setpoints for the Reactor Water Cleanup penetration 
    room steam leak detection function.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability [of occurrence] [sic] or consequences of an 
    accident evaluated.
        FSAR section 5.2.5.1.3 addresses the ambient and differential 
    room ventilation temperature leakage detection. This section states:
        ``...switch setpoints are based on the temperature rise 
    resulting from a leak at system conditions corresponding to full 
    reactor power.''
        NRC Safety Evaluation on the RWCU system steam leak detection 
    system (related to Amendment Number 123 to License NPF-14 and 
    Amendment Number 90 to License NPF-22) reviewed and found acceptable 
    the PP&L criteria for calculating the leak detection setpoints for 
    the RWCU system, which include:
        1. Setpoints are selected to detect and isolate a leak that is 
    normally less than 25 gpm and below the flow rate corresponding for 
    the critical crack size for the system piping.
        2. Setpoints are set high enough to avoid inadvertent isolation 
    caused by normal temperature transients or abnormal transients 
    caused by non-leak conditions (such as loss of ventilation).
        This NRC SER also stated that a leak rate of 25 gpm is less than 
    those leak rates associated with the onset of unstable pipe 
    ruptures. This fact is also shown in FSAR figure 5.2-10. This value 
    of 25 gpm constitutes the design basis for the steam leak detection 
    system.
        The mixing and liquid energy addition assumption changes in the 
    analysis do not affect this design basis. The analysis calculates 
    the resulting room temperature increase from a 25 gpm leak. In fact, 
    the new assumptions provide a more accurate yet conservative 
    prediction of room temperature increases. Therefore, operation of 
    the system is improved.
    
    [[Page 64390]]
    
        The proposed change leads to higher calculated room temperatures 
    to be used in the differential temperature setpoint calculations. 
    The engineering study was reviewed to determine if the higher 
    calculated temperatures would have a negative impact on the High 
    Energy Line Break and Leak Analysis environmental study which 
    provides the basis for equipment qualification.
        In determining the room temperatures, the engineering study 
    considers ambient temperature setpoints at which the leaks will be 
    isolated. The proposed action will not change the ambient 
    temperature setpoints, and actuation of these instruments will 
    ensure that the results of the engineering study will not be 
    adversely affected. Therefore, no impact on equipment qualification 
    is being introduced by this change.
        FSAR chapter 15 was reviewed for potential impacts on the 
    accident analyses. The 25 gpm leak outside containment is not 
    specifically analyzed in FSAR chapter 15. However, other conditions 
    which result in coolant leakage outside containment are analyzed in 
    section 15.6.2 (Instrument Line Break) and 15.6.4 (Steam System 
    Piping Break Outside Containment). As stated in the NRC SER, the 25 
    gpm RWCU leak rate is bounded by the analysis in FSAR section 
    15.6.4. FSAR section 15.6.2 also states that leak detection 
    actuations will initiate operator actions, a fact that is not 
    affected by the proposed change. Therefore, based on a review of 
    FSAR chapter 15 it was concluded that no impact on the analyzed 
    accident scenarios is created by the proposed change.
        Based on the above discussions, it is demonstrated that the 
    proposed change will not adversely impact system function or 
    equipment. System performance will actually be improved since the 
    new setpoints eliminate spurious isolations resulting from a less 
    accurate model. The setpoint change has no impact on any equipment 
    important to safety or any accidents previously analyzed in the 
    FSAR. Therefore, the proposed change does not involve a significant 
    increase in the probability of occurrence or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed action does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    Neither the system design basis nor the system function will be 
    adversely affected. System performance will be enhanced since 
    spurious differential temperature actuations will be reduced as a 
    result of using the more accurate, yet conservative, COTTAP model. 
    In addition to this, redundant temperature isolation function will 
    continue to be provided by the existing high ambient temperature 
    detectors.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed action does not involve a significant reduction in 
    a margin of safety. The Technical Specification basis for the 
    setpoints is to detect a leak below the flow rate corresponding to 
    critical crack size for the system piping. As stated previously, the 
    25 gpm flow rate is an acceptable flow rate and is used to calculate 
    the new temperatures.
        Although the newly calculated RWCU penetration room temperatures 
    will be higher (due to the improved model), the isolation actuation 
    will be initiated by the high ambient temperature detectors before 
    the penetration room temperatures reach the newly calculated values, 
    as would happen under the old model. Therefore, system response is 
    not adversely affected.
        The current temperature values lead to differential temperature 
    setpoints which are too low, causing spurious isolations. The use of 
    the new temperature values will reduce the number of spurious 
    isolations, reducing unnecessary challenges to safety systems during 
    normal plant operations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: September 18, 1995
        Description of amendment request: The proposed Technical 
    Specifications (TS) changes would revise TS Table 4.3.1.1-1, ``Reactor 
    Protection System Instrumentation Surveillance Requirements'' to 
    reflect the change in the calibration frequency for the Local Power 
    Range Monitor (LPRM) signal from every 1000 Effective Full Power Hours 
    (EFPH) to every 2000 Megawatt Days per Standard Ton (MWD/ST).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The change in the calibration frequency of the Local Power Range 
    Monitor (LPRM) signal does not make any physical change to the fuel 
    or the manner in which the fuel responds to a transient or accident. 
    The proposed TS change does not affect the fundamental method by 
    which the LPRMs are calibrated. Also, the LPRM calibration frequency 
    is not considered an initiator of any events analyzed in the SAR. 
    Therefore, calibrating the LPRMs on a different frequency will not 
    increase the probability of occurrence of an accident previously 
    evaluated in the SAR.
        The resulting nodal power uncertainty does not exceed the nodal 
    power uncertainty accounted for in the existing Minimum Critical 
    Power Ratio (MCPR) Safety Limit; thus, the MCPR Safety Limit is not 
    affected by this TS Change, and, therefore, the initial conditions 
    of any accident are unchanged. Since the calibration frequency 
    change will not affect the course of any evaluated accident, the 
    consequences of an accident previously evaluated in the SAR will not 
    be increased.
        Therefore, the proposed TS change does not involve an increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The change in the calibration frequency of the Local Power Range 
    Monitor (LPRM) signal does not make any physical change to the plant 
    or the manner in which the equipment responds to a transient or 
    accident. The proposed TS change does not introduce a new mode of 
    plant operation and does not involve the installation of any new 
    equipment or instrumentation. The fuel will continue to be operated 
    to the same safety limits since the Minimum Critical Power Ratio 
    (MCPR) Safety Limit remains unchanged due to this TS change.
        Therefore, the proposed TS change does not create the 
    possibility of a new or different kind of accident, from any 
    accident previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        The following TS Bases were reviewed for potential reduction in 
    the margin of safety:
        2.0 Safety Limits and Limiting Safety System Settings;
        3/4.1 Reactivity Control Systems;
        3/4.2.1 Average Planar Linear Heat Generation Rate;
        3/4.2.3 Minimum Critical Power Ratio:
        3/4.2.4 Linear Heat Generation Rate;
        3/4.3.1 Reactor Protection System Instrumentation;
        3/4.3.6 Control Rod Block Instrumentation;
        3/4.3.7.7 Traversing In-Core Probe System;
        The GE Thermal Analysis Basis (GETAB) determination of the 
    Minimum Critical Power Ratio (MCPR) Safety Limit allows a maximum 
    total nodal uncertainty of the Traversing In-Core Probe (TIP) 
    readings of which the Local Power Range Monitor (LPRM).
        Update uncertainty is a part. The change in LPRM calibration 
    frequency results in an LPRM Update uncertainty which, when combined 
    with the other uncertainties which comprise the total TIP readings 
    uncertainty, yields a total TIP readings nodal power uncertainty of 
    less than the allowed GETAB uncertainty. Thus the change in LPRM
    
    [[Page 64391]]
    
    calibration frequency will not affect the MCPR Safety Limit.
        The LPRMs are utilized as input to the Average Power Range 
    Monitor (APRM) and Rod Block Monitor (RBM) systems. The primary 
    safety function of the APRM system is to initiate a scram during 
    core-wide neutron flux transients before the actual core-wide 
    neutron flux level exceeds the safety analysis design basis. This 
    prevents fuel damage from single operator errors or equipment 
    malfunctions. The APRMs are calibrated at least once per week to the 
    plant heat balance, utilize a radially and axially diverse group of 
    LPRMs as input and are utilized to detect changes in average, not 
    local, power changes. Therefore, the effects of changing the LPRM 
    calibration frequency on the APRM system responses will be minimal 
    due to any individual LPRM drift being practically canceled out (due 
    to diversity of input) and/or due to the frequent recalibration of 
    the APRMs to an independent power calculation (the heat balance). 
    Thus, changing the LPRM calibration frequency will not impact the 
    capability of the APRM system to perform the scram function, and 
    there is no impact on transient delta-CPRs.
        The RBM system is utilized in the mitigation of a Rod Withdrawal 
    Error (RWE) event. The RBM system is designed to prevent the 
    operator from increasing the local power significantly when 
    withdrawing a control rod. Under Average Power Range Monitor - Rod 
    Block Monitor Technical Specifications/Maximum Extended Load Line 
    Limit Analysis (ARTS/MELLLA) on each selection of a control rod, the 
    average of the assigned, unbypassed LPRMs is adjusted to equal a 
    100% reference signal for each of the two RBM channels. Each RBM 
    channel automatically limits the local thermal margin changes by 
    limiting the allowable change in local average neutron flux to the 
    RBM setpoint. If the local average neutron flux change is greater 
    than that allowed by the RBM setpoint, within either RBM channel, 
    the rod withdrawal permissive is removed preventing further rod 
    movement. Since the change in local neutron flux is calculated from 
    the change in the average of the LPRM readings, and calibrated on 
    every rod selection to the reference signal, offsets in individual 
    LPRM readings due to calibration differences are effectively 
    eliminated for a given RBM setpoint. Therefore, the constraints on 
    the withdrawal of any given rod are unchanged, and there will not be 
    any increase in RWE delta-CPR.
        Since the MCPR Safety Limit is unaffected and the delta-CPR 
    values are unchanged, the cycle CPR Operating limits are unchanged 
    due to this TS change. Therefore, the proposed change in the 
    frequency of LPRM signal calibration does not result in a reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, PA 19101
        NRC Project Director: John F. Stolz
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: May 3, 1996
        Description of amendment request: The proposed Technical 
    Specifications (TS) changes would revise TS Surveillance Requirements 
    4.6.5.3.a and 4.6.5.4.a to modify specific requirements to perform 
    surveillance flow testing of the Standby Gas Treatment and Reactor 
    Enclosure Recirculation Systems from monthly to quarterly.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS changes do not involve any physical changes to 
    plant systems or equipment. The proposed TS changes only change the 
    Surveillance Requirements (SRs) surveillance test frequency 
    pertaining to flow testing of the SGTS and RERS from monthly to 
    quarterly. The periodic surveillance test frequencies provide 
    adequate assurance that the equipment tested will remain in an 
    operable condition. The test frequency interval for the flow testing 
    of the SGTS and RERS was determined from the regulatory position in 
    USNRC Regulatory Guide 1.52, ``Design, Testing, and Maintenance 
    Criteria for Post Accident Engineered-Safety-Feature Atmosphere 
    Clean-up System Air Filtration and Adsorption Units of Light-Water-
    Cooled Nuclear Power Plants''. As stated in Regulatory Position 
    C.4.d, ''... each Engineered Safety Feature (ESF) atmosphere cleanup 
    train should be operated at least 10 hours per month, with the 
    heaters on (if so equipped), in order to reduce the buildup of 
    moisture on the absorbers and HEPA filters.''
        System operation on a monthly basis for the purpose of 
    preventing moisture buildup on the absorbers as described in R.G. 
    1.52 is not required at Limerick due to the continuous dry 
    instrument air purge described previously in the Safety Assessment 
    section of this submittal. Therefore a change in the interval 
    between tests from monthly to quarterly will not result in moisture 
    accumulation which would reduce the capability of the absorber to 
    remove the iodine species from the exhaust air flow stream.
        The SGTS components are common to both units and must be run 
    with the associated RERS for the surveillance test for each unit. 
    The currently specified test frequency results in the SGTS being run 
    at least twice per month or as many as eight (8) times per quarter 
    for this surveillance, in addition to other required system 
    surveillance tests which require the use of the components in this 
    system. A change in surveillance test frequency from monthly to 
    quarterly would reduce the wear on system components and thereby 
    reduce the associated system downtime for maintenance and repairs. 
    The consequent increased availability provides greater assurance 
    that the system will be able to perform its mitigation function 
    following any postulated accident.
        Surveillance test frequency on a quarterly interval is 
    considered adequate to verify operability, as demonstrated by the 
    required quarterly test interval for other equipment important to 
    safety which have a similar function, such as the requirement for 
    quarterly verification of the isolation time of the secondary 
    containment and refueling area isolation valves, as required by LGS 
    TS Sections 4.6.5.2.1 and 4.6.5.2.2.
        Therefore, the proposed TS changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes only involve changes to the frequency in 
    which the specified surveillances tests are performed. The proposed 
    TS changes do not physically change the design or intended function 
    of the systems, structures, or components associated with the SGTS 
    or RERS. There will be no change to the existing redundancy of 
    systems and components. The proposed change in surveillance test 
    frequency will not introduce the possibility of any failure 
    mechanisms of a different type than those already evaluated in the 
    SAR. The existing components will not be used in any different 
    manner and no new components will be added. Therefore with no 
    physical changes and no new or different manner of system operation, 
    no new failure mechanisms or equipment failure modes are created.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety as defined in the LGS TS Bases has not been 
    reduced. The specific basis for the 31 day surveillance interval is 
    not given in the LGS TS Bases section nor in the LGS UFSAR Sections 
    6.5.1 or 9.4.2 which discuss the subject systems. However, 
    Regulatory Position C.4.d of Regulatory Guide 1.52, Revision 2, 
    relating to maintenance requirements, recommends:
        Each ESF atmosphere cleanup train should be operated 
    at least 10 hours per month, with the heaters on (if so equipped), 
    in order to reduce the buildup of moisture on the absorbers and HEPA 
    filters.''
    
    [[Page 64392]]
    
        The Bases for Surveillance Requirements (SR) 3.6.4.3.1 in the 
    Standard Technical Specifications for General Electric Plants, BWR/
    4, which corresponds to the subject LGS TS test, also notes the need 
    for ten (10) hours of operation per month for elimination of 
    moisture in the filters.
        The basis for the requirement for a monthly test with the 
    heaters energized is clearly related to the desired elimination of 
    moisture in the filters and absorbers. However, LGS UFSAR Table 6.5-
    2 states that LGS does not conform to R.G. 1.52, Position C.4.d 
    because the SGTS and RERS trains are ``continuously purged with dry 
    instrumentation air to prevent build-up of moisture.'' UFSAR 
    Sections 6.5.1.1.2 and 6.5.1.3.2 provide additional discussion of 
    this method of moisture control.
        Therefore, the proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, PA 19101
        NRC Project Director: John F. Stolz
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: September 27, 1996
        Description of amendment request: The proposed Technical 
    Specifications (TS) changes would increase the Reactor Enclosure 
    Secondary Containment maximum inleakage rate. This change will also 
    impact secondary containment drawdown time and system flow rate 
    assumptions, thereby, affecting charcoal filter bed efficiency and post 
    accident dose analysis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Changing the Reactor Enclosure post drawdown inleakage rate from 
    1250 cfm to 2500 cfm does not involve any changes to the function or 
    operation of any plant component or safety related system. The 
    Reactor Enclosure Recirculation System (RERS) and the Standby Gas 
    Treatment System (SGTS) will maintain their design function by 
    mitigating the radiological consequences of the analyzed accident 
    and mitigating the post LOCA temperatures within the Reactor 
    Enclosures. No analyzed accident initiating events are impacted, no 
    new accident initiators are created, and no new failure modes are 
    created. There are no changes to the redundancy, separation, quality 
    assurance or fire protection requirements for the associated 
    components and systems.
        The proposed changes to the LGS adsorber bed residence time will 
    no longer fully meet the literal design guidance provided in 
    Regulatory Guide (RG) 1.52, ``Design, Testing, and Maintenance 
    Criteria for Post Accident Engineered-Safety-Feature Atmosphere 
    Cleanup System Air Filter and Adsorption Units of Light-Water-Cooled 
    Nuclear Power Plants,'' Revision 2, March 1978. This is because 
    LGS's unique, yet more conservative, adsorber bed design is not 
    addressed by the RG residence time design guidance. However, the LGS 
    SGTS charcoal adsorbers still conform to the design function 
    described in RG 1.52, based on the following: The LGS design with 
    increased inleakage will continue to conform to the three conditions 
    specified by RG 1.52, Position C.6.a, in order to maintain an 
    assigned decontamination efficiency of 99%; there is a conservative 
    amount of charcoal adsorber material provided by the LGS design, 
    based on calculations performed in accordance with RG 1.3 
    ``Assumptions Used For Evaluating The Potential Radiological 
    Consequences of a Loss of Coolant Accident For Boiling Water 
    Reactors; and the LGS charcoal bed design is more conservative than 
    the RG 1.52 design guidance, based on data (i.e., Iodine Penetration 
    vs. Air Velocity) published by the charcoal manufacturer.
        Therefore, the probability of occurrence and the consequences of 
    a malfunction of equipment important to safety is not increased. 
    Also, the probability of occurrence of an accident previously 
    evaluated is not increased. However, the proposed changes do affect 
    the leak tightness of the Unit 1 and Unit 2 Reactor Enclosure, which 
    increases the consequences of a postulated accident previously 
    evaluated.
        Changing the Reactor Enclosure post drawdown inleakage rate from 
    1250 cfm to 2500 cfm will result in an increase in the calculated 
    LOCA/LOOP Design Basis Accident (DBA) off-site and on-site doses. 10 
    CFR Part 100, and 10 CFR Part 50 Appendix A, General Design Criteria 
    (GDC) 19, establish reference dose values used to determine site 
    suitability and provide reasonable assurance that the facility can 
    be operated following the analyzed accident without undue risk to 
    the health and safety of the public. The proposed TS changes will 
    increase the SGTS drawdown time from 2 minutes and 20 seconds to 15 
    minutes and 30 seconds. The drawdown time increase will not prevent 
    the RERS/SGTS from performing all of their safety related functions. 
    However, because it is conservatively assumed that all radioactive 
    material released during the drawdown period is unfiltered, and 
    because the drawdown period has been extended whereby more 
    unfiltered radioactive material is assumed to be released following 
    the DBA, there is a corresponding increase in the calculated 
    Exclusion Area Boundary (EAB), Low Population Zone (LPZ), and 
    Control Room doses. It is also assumed that the SGTS exhausts at the 
    maximum inleakage rate throughout the entire DBA evaluation period 
    (i.e., 30 days) where an increase in the maximum inleakage rate 
    would also contribute to higher postulated EAB, LPZ, and Control 
    Room doses. However, the proposed calculated doses do not exceed 10 
    CFR Part 100, or 10 CFR Part 50, Appendix A, DGC 19 reference doses.
        Since the proposed doses resulting from the changes remain below 
    10 CFR Part 100, and 10 CFR Part 50, Appendix A, these proposed 
    changes will not significantly increase the consequences of an 
    accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Changing the Reactor Enclosure post drawdown inleakage rate from 
    1250 cfm to 2500 cfm is not an accident initiator nor does it result 
    in the occurrence of an accident. The changes do not affect the 
    function or operation of any plant component or safety related 
    system nor do they create any new failure modes.
        In addition, the proposed changes do not involve any changes to 
    the function or operation of any plant system or component nor will 
    they adversely affect the Reactor Enclosure post LOCA environmental 
    conditions. Furthermore, these changes will not create any new or 
    different failure modes for the equipment important to safety within 
    the Reactor Enclosure Secondary Containment.
        Therefore, the possibility of an accident of a different type or 
    a different type of malfunction of equipment important to safety 
    than previously evaluated is not created.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        Changing the Reactor Enclosure post drawdown inleakage rate from 
    1250 cfm to 2500 cfm will result in reducing the margin of safety as 
    defined in the LGS Updated Final Safety Analysis Report (UFSAR) 
    relative to the off-site and on-site doses following a LOCA/LOOP 
    DBA, and an increase of the UFSAR specified system drawdown time. 
    From a system perspective, increasing the SGTS drawdown time from 2 
    minutes and 20 seconds to 15 minutes and 30 seconds will not prevent 
    the RERS/SGTS from performing all of their safety related functions. 
    There will be a postulated increase in the corresponding EAB, LPZ, 
    and Control Room doses, since it is assumed that fuel damage occurs 
    coincident with the LGS DBA (i.e, at time = 0), all radioactive 
    material released during the drawdown time is unfiltered, and the 
    drawdown time is proposed to be extended whereby more unfiltered 
    radioactive material could be released. It is also assumed that the 
    SGTS exhausts at the maximum inleakage rate throughout the entire 
    DBA evaluation period (i.e., 30 days) where an increase in the 
    maximum inleakage
    
    [[Page 64393]]
    
    rate would also contribute to higher postulated EAB, LPZ, and 
    Control Room doses. However, these calculated doses will remain 
    below 10 CFR Part 100, and 10 CFR Part 50, Appendix A, GDC 19 
    reference doses.
        Therefore, these proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, PA 19101
        NRC Project Director: John F. Stolz
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: October 1, 1996
        Description of amendment request: The proposed amendment would 
    allow for a one-time extension of the surveillance intervals for the 
    containment isolation valve (CIV) seat leakage test, the isolation 
    valve seal water test, the boron injection tank leakage test, the 
    containment spray nozzle test, and the city water backup to the 
    auxiliary boiler feed pump test. These tests would be performed during 
    the refueling outage scheduled to begin in April 1997.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Regarding the Containment Isolation Valve seat leakage and 
    Isolation Valve Seal Water tests:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response:
        The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The probability of a previously evaluated accident will 
    not increase because CIV leakage does not provide any role in 
    accident initiation. The CIVs provide containment isolation 
    following a design basis accident.
        The consequences of an accident previously evaluated will not 
    significantly increase because the CIV leakage measurements contain 
    significant margin to a more restrictive criteria based on the 
    requested surveillance interval extension. As discussed in Section 
    II, ``Evaluation of Changes,'' [see application dated October 1, 
    1996] based on an evaluation of past CIV leak tests, the proposed 
    change will not result in an increase in containment leakage because 
    the measured leakage in previous CIV leak tests shows large margin 
    to a more restrictive criteria based on the requested surveillance 
    interval extension. Also, the latest test of IVSWS [isolation valve 
    seal water system] satisfied the established acceptance criteria.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response:
        The proposed license amendment does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated. The proposed change only provides for a relatively short, 
    one-time extension of the current leak-test interval for certain 
    containment isolation valves. The proposed change does not involve 
    the addition of any new or different type of equipment, nor does it 
    involve operating equipment required for safe operation of the 
    facility in a manner different from that addressed in the Final 
    Safety Analysis Report. Therefore, the proposed change will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        The proposed amendment does not involve a significant reduction 
    in a margin of safety. The proposed change, for a one-time extension 
    of the test interval, will not result in a significant reduction in 
    a margin of safety because the test interval is being extended by 
    only a short period and the measured leakage in previous CIV leak 
    tests shows large margin to a more restrictive criteria based on the 
    surveillance interval extension. In addition, the online leakage 
    monitoring capability of the WCCPPS [weld channel containment 
    penetration pressurization system] helps ensure that changes in CIV 
    leakage during the extension period will be detected. Therefore, 
    this change does not create a significant reduction in a margin of 
    safety.
        Regarding the Boron Injection Tank (BIT) leakage test:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response:
        The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The proposed change will not degrade the 
    integrity of the BIT piping outside containment because no time 
    dependent failure trends were observed in the review of past test 
    results. The probability of a previously evaluated accident will not 
    be increased because BIT leakage does not provide any role in 
    accident prevention. The BIT leakage test only verifies that the BIT 
    and associated piping meet specified leakage limits.
        The consequences of an accident previously evaluated will not 
    significantly increase because the BIT leakage test results show 
    large margins to the allowable leakage limit.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response:
        The proposed license amendment does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated. The proposed change does no[t] involve the addition of 
    any new or different type of equipment, nor does it involve 
    operating equipment required for safe operation of the facility in a 
    manner that's different from that addressed in the Final Safety 
    Analysis Report. Also, the increased surveillance interval (one-time 
    only) will not adversely affect the integrity of the BIT piping and 
    will not result in any new failure modes. Therefore, the proposed 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        The proposed license amendment does not involve a significant 
    reduction in a margin of safety. Because of the large margin between 
    the previous test and the allowable leak rate limit, the proposed 
    change, for a one-time extension of the test interval, for the BIT 
    leakage test does not adversely affect the performance of any safety 
    related system, component, and does not result in increased severity 
    of any of the accidents considered in the Final Safety Analysis 
    Report. Based on past test results, the one-time extension of the 
    leak test interval does not involve a significant reduction in a 
    margin of safety.
        Regarding the Containment Spray Nozzle test:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response:
        The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. As discussed in Section II, ``Evaluation of 
    Changes,'' [see application dated October 1, 1996] based on an 
    evaluation of past test results the proposed change will not degrade 
    the reliability of the Containment Spray Nozzles because no time 
    dependent failure trends were observed in the data review. The 
    probability of a previously evaluated accident will not be increased 
    because the Containment Spray Nozzles do not provide any role in 
    accident prevention. The Containment Spray Nozzles provide a uniform 
    spray distribution for containment cooling following postulated 
    post-accident conditions.
        The consequences of an accident previously evaluated will not 
    increase because the Containment Spray Nozzle reliability is not 
    degraded by this change.
    
    [[Page 64394]]
    
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response:
        The proposed license amendment does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated. The proposed change does not involve the addition of any 
    new or different type of equipment, nor does it involve operating 
    equipment required for safe operation of the facility in a manner 
    that is different from that addressed in the Final Safety Analysis 
    Report. Also, the increased surveillance interval (one-time only) 
    w[i]ll not adversely affect the functioning of the Containment Spray 
    Nozzles and will not result in any new failure modes. Therefore, the 
    proposed change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        The proposed license amendment does not involve a significant 
    reduction in a margin of safety. The proposed change, for a one-time 
    extension of the test interval, for the Containment Spray Nozzles 
    does not adversely affect the performance of any safety related 
    system, component, or instrument, or safety system setpoints and 
    does not result in increased severity of any of the accidents 
    considered in the Final Safety Analysis Report. Based on past test 
    results, the one-time extension of the functional test interval will 
    not adversely affect the functioning of the Containment Spray 
    Nozzles. Therefore, this change does not create a significant 
    reduction in a margin of safety.
        Regarding the City Water Backup test:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response:
        The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The proposed change will not degrade the 
    reliability of the City Water Backup Supply Valves for the AFW 
    [auxiliary feedwater] System because no time dependent failure 
    trends were observed in the review of past test results. The 
    probability of a previously evaluated accident will not increase 
    because the City Water Backup Supply Valves for the AFW System do 
    not provide any role in accident prevention. The City Water Backup 
    Supply Valves for the AFW System only provides a diverse source of 
    water for the AFW system.
        The consequences of an accident previously evaluated will not 
    significantly increase because the City Water Backup Supply Valves 
    for the AFW System are not assumed to function to mitigate any 
    analyzed accident.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response:
        The proposed license amendment does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated. The proposed change does not involve the addition of any 
    new or different type of equipment, nor does it involve operating 
    equipment required for safe operation of the facility in a manner 
    that is different from that addressed in the Final Safety Analysis 
    Report. Also, the increased surveillance interval (one-time only) 
    will not adversely affect the functioning of the City Water Backup 
    Supply Valves for the ABFP [auxiliary boiler feedpump] and will not 
    result in any new failure modes. Therefore, the proposed change will 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        The proposed amendment does not involve a significant reduction 
    in a margin of safety. The proposed change, for a one-time extension 
    of the test interval, for the City Water Backup Supply Valves for 
    the ABFP does not adversely affect the performance of any safety 
    related system, component, or instrument, or safety system setpoints 
    and does not result in increased severity of any of the accidents 
    considered in the Final Safety Analysis Report. Based on past test 
    results, the one-time extension of the functional test interval will 
    not adversely affect the functioning of the City Water Backup Supply 
    Valves for the AFW System. Therefore, this change does not create a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: S. Singh Bajwa, Acting
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: October 25, 1996
        Description of amendment request: The proposed change to Hope Creek 
    Technical Specification (TS) 3/4.1.3.5, ``Control Rod Scram 
    Accumulator'', would: 1) permit a separate entry into a Technical 
    Specification action statement for each inoperable control rod; 2) 
    provide more specific applicability for required actions in operational 
    condition 1 or 2 with one inoperable control rod scram accumulator 
    (reactor pressure of greater than or equal to 900 psig would be 
    specified); 3) provide more specific actions (verify charging water 
    pressure) for two or more inoperable control rod scram accumulators and 
    reactor pressure is greater than or equal to 900 psig; 4) provide more 
    specific actions when reactor pressure is less than 900 psig and one or 
    more control rod scram accumulators are inoperable (verify insertion of 
    control rods associated with inoperable accumulators and verify that 
    charging water header pressure is greater than or equal to 940 psig); 
    and 5) provide specific actions in operational condition 5 with one or 
    more withdrawn control rods inoperable; and 6) eliminate the 
    requirements to perform a 18-month channel functional test of the leak 
    detectors and the 18-month channel calibration of the pressure 
    detectors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The change incorporates the appropriate content of the improved 
    BWR/4 Standard Technical Specifications, NUREG-1433, for Control Rod 
    Scram Accumulators.
        The proposed Technical Specification and required Action 
    completion times are consistent with or more conservative than those 
    approved for use in the improved Technical Specifications for 
    inoperable control rod scram accumulators. In addition, the proposed 
    surveillance requirements for the control rod scram accumulators are 
    sufficient to adequately demonstrate operability as stated in the 
    Bases for the improved Technical Specifications. Further, the 
    proposed changes enhance the current Hope Creek Technical 
    Specifications by reflecting improved techniques collectively 
    learned by the industry. Therefore, the proposed changes do not 
    significantly increase the risk or consequences of any accidents 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Neither the mechanism for initiating or completing a scram is 
    modified by this proposed change. There are no physical changes to 
    plant equipment proposed in the application. The proposed change 
    does not create a means by which the scram function could be impeded 
    or prevented. The proposed change is functionally equivalent to the 
    current Technical Specifications, but provides additional 
    operational flexibility to diagnose and resolve equipment issues 
    that do not impact operability of the control rods before taking 
    proscriptive actions which
    
    [[Page 64395]]
    
    result in significant plant transients (i.e. full power scram).
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The operability of the accumulators and the scram function of 
    the control rod drive system protects the Safety Limit Minimum 
    Critical Power Ratio as well as the 1% cladding plastic strain fuel 
    design limit. The proposed change does not reduce a margin of safety 
    as defined in the Bases of the Technical Specification since the 
    proposed change does not affect the maximum allowable scram times 
    for control rods, nor does it change the maximum allowable number or 
    minimum separation of inoperable control rods. The proposed change 
    does not modify any instrument setpoints or functions. The proposed 
    change will either maintain the present margins of safety or 
    increase them, by reducing the need for unnecessary challenges to 
    the reactor protection system and resulting plant shutdowns, while 
    still maintaining the capability to complete a reactor scram.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: October 29, 1996
        Description of amendment request: The proposed amendment would 
    revise the mode of applicability for the motor-driven auxiliary 
    feedwater (AFW) pump actuation on opening of the main feedwater (MFW) 
    pump breakers to correct an error introduced during Amendment No. 61.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The less restrictive changes discussed in Section C.1 [of the 
    licensee's application] do not involve a significant hazards 
    consideration as discussed below:
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated. The proposed 
    changes only correct an error which was introduced in Amendment No. 
    61 to the Ginna Station technical specifications. The changes revert 
    the mode of applicability for the motor-driven AFW pump actuation on 
    the opening of the MFW pump breakers to what existed previously. The 
    change is essentially correction of a typographical error that was 
    caused through use of the electronic version of NUREG-1431 in 
    preparation of the Ginna Station ITS [Improved Technical 
    Specifications]. There have been no subsequent plant modifications 
    or changes to the accident analysis which would invalidate the 
    previous NRC acceptance of only requiring this Function above 5% 
    power. The accident analyses do not credit automatic initiation of 
    AFW on MFW pump trip in MODE 2. As such, these changes do not impact 
    initiators or analyzed events or assumed mitigation of accident or 
    transient events. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously analyzed.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The proposed changes 
    do not involve a physical alteration of the plant (i.e., no new or 
    different type of equipment will be installed) or changes in the 
    methods governing normal plant operation which existed prior to 
    Amendment No. 61. The proposed changes will not impose any new or 
    different requirements. Thus, this change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety. The proposed changes will not reduce a margin of plant 
    safety because there have been no subsequent plant modifications or 
    changes to the accident analysis which would invalidate the previous 
    NRC acceptance of only requiring this Function above 5% power. As 
    such, no question of safety is involved, and the change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005
        NRC Project Director: S. Singh Bajwa, Acting
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: October 29, 1996
        Description of amendment request: The proposed amendment would 
    revise the Required Actions for the auxiliary feedwater (AFW) pump 
    actuation on Steam Generator Level (SG) - Low Low logic to be 
    consistent with those specified in NUREG-1431.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The less restrictive changes discussed in Section C.1 [of the 
    licensee's application] do not involve a significant hazards 
    consideration as discussed below:
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated. The proposed 
    changes with respect to the Required Actions for AFW actuation on SG 
    Level - Low Low logic provide consistency with NUREG-1431 by 
    requiring an inoperable channel to be placed in the tripped 
    condition within 6 hours. The affected logic then requires 1 of 2 
    channels in order to actuate such that there is no impact on any 
    initiators or analyzed events or assumed mitigation of accident or 
    transient events. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously analyzed.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The proposed 
    changes do not involve a physical alteration of the plant (i.e., no 
    new or different type of equipment will be installed) or changes in 
    the methods governing normal plant operation. The proposed changes 
    will not impose any new or different requirements. Thus, this change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety. The proposed changes will not reduce a margin of plant 
    safety because the AFW actuation on SG Level - Low Low still remains 
    capable of performing its function with an inoperable channel placed 
    in the tripped configuration. These changes are also consistent with 
    those provided in NUREG-1431. As such, no question of safety is 
    involved, and the change does not involve a significant reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three
    
    [[Page 64396]]
    
    standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location:  Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005
        NRC Project Director: S. Singh Bajwa, Acting
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: September 4, 1996
        Description of amendment request: The proposed amendment to the 
    Technical Specifications would allow the use of four lead test 
    assemblies (advanced zirconium-based alloys) in the North Anna, Units 1 
    and 2, reactor cores.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the four FCF [Framatome Cogema Fuels] lead test 
    assemblies will not:
        1.Involve a significant increase in the probability of 
    occurrence or the consequences of an accident previously evaluated. 
    The FCF lead test assemblies are very similar in design to the 
    Westinghouse fuel that comprises the remainder of the core. The 
    reload core design for North Anna cycles which incorporate the lead 
    test assemblies will meet all applicable design criteria. In 
    addition, the performance of the ECCS [emergency core cooling 
    system] at North Anna Units 1 and 2 will not be affected by the 
    insertion of the four lead test assemblies, so the criteria of 10 
    CFR 50.46 will be satisfied for use of these assemblies with fuel 
    rods, guide thimble tubes, and instrumentation tubes fabricated with 
    advanced zirconium-based alloys. The use of these fuel assemblies 
    will not result in a change to the North Anna Units 1 and 2 reload 
    design and safety analysis limits. The existing safety analyses 
    based on the resident Westinghouse fuel will remain applicable for 
    cycles which incorporate the lead test assemblies. Therefore, 
    neither the probability of occurrence nor the consequences of any 
    accident previously evaluated is significantly increased.
        2. Create the possibility for a new or different type of 
    accident from any accident previously evaluated. The FCF lead test 
    assemblies are very similar in design (both mechanical and 
    composition of materials) to the resident Westinghouse fuel. North 
    Anna cores which incorporate the lead test assemblies will be 
    designed to meet all applicable design criteria and ensure that all 
    pertinent licensing basis criteria are met. Demonstrated adherence 
    to these standards and criteria precludes new challenges to 
    components and systems that could introduce a new type of accident. 
    North Anna safety analyses based on the resident Westinghouse fuel 
    will remain applicable for cores containing the lead test 
    assemblies. All design and performance criteria will continue to be 
    met and no single failure mechanisms have been created. In addition, 
    the use of these fuel assemblies does not involve any alteration to 
    plant equipment or procedures which would introduce any new or 
    unique operational modes or accident precursors. Therefore, the 
    possibility for a new or different kind of accident from any 
    accident previously evaluated is not created.
        3. Involve a significant reduction in the margin of safety. The 
    use of the FCF lead test assemblies does not change the performance 
    requirements on any system or component such that any design 
    criteria will be exceeded, and will not cause the core to operate in 
    excess of pertinent design basis operating limits. North Anna reload 
    core designs for cycles which incorporate the lead test assemblies 
    will specifically evaluate any pertinent differences between the 
    lead test assemblies and the resident fuel, and will take into 
    consideration the normal core operating conditions allowed in the 
    Technical Specifications. Safety analyses based on the resident 
    Westinghouse fuel will remain applicable for cores incorporating the 
    FCF lead test assemblies. Analyses or evaluations will be performed 
    each cycle to confirm that the criteria in 10 CFR 50.46 will be met. 
    Therefore, the margin of safety as defined in the Bases to the North 
    Anna Units 1 and 2 Technical Specifications is not significantly 
    reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Acting Project Director: Mark Reinhart
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: November 6, 1996
        Description of amendment request: The proposed changes will modify 
    the requirements for isolated loop startup to permit filling of a 
    drained isolated loop via backfill from the reactor coolant system 
    through partially open stop loop valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of the North Anna Power Station [in] 
    accordance with the proposed changes will not:
        1. Involve a significant increase in the probability of 
    occurrence or consequences of an accident previously evaluated. The 
    probability of occurrence of a positive reactivity addition accident 
    is not being increased by the proposed Technical Specification 
    change. The proposed restrictions on boron concentration and mixing, 
    reactor coolant system inventory and reactivity and count rate 
    monitoring provide a level of protection against reactivity addition 
    accidents which is equivalent to that currently in place.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated. The proposed change does not 
    introduce any new or unique failure modes or accident precursors. 
    Eliminating the operability requirements for the loop stop valve 
    interlocks does not create any new or different kind of accident 
    scenario. Loop startup accidents in the various modes of operation 
    have been analyzed. Operation of the loop stop valves will not 
    change. New requirements have been imposed for the case of 
    backfilling a drained loop from the reactor coolant system to ensure 
    that core cooling and reactivity control are preserved throughout 
    the backfill evolution.
        3. Involve a significant reduction in any margin of safety. The 
    new Technical Specification loop isolation and startup requirements 
    for temperature, boron concentration, and shutdown margin fulfill 
    the function of the loop stop valve interlocks. Therefore, the 
    margin of safety as defined in any Technical Specification bases is 
    not reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Mark Reinhart (Acting)
    
    [[Page 64397]]
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: October 31, 1996
        Description of amendment request: The proposed amendment would 
    revise the Kewaunee Nuclear Power Plant (KNPP) Technical Specifications 
    (TS) by deleting the requirement for an annual submittal of a 
    description of changes made pursuant to 10 CFR 50.59. Consistent with 
    10 CFR 50.59(b)(2), a description of changes will subsequently be 
    included with the KNPP Updated Safety Analysis Report (USAR) update in 
    accordance with 10 CFR 50.71(e). Additionally, the proposed amendment 
    would correct minor administrative inconsistencies in the TS Table of 
    Contents and in a footnote reference.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c)The NRC staff's review is 
    presented below:
        On August 31, 1992 (57 FR 39353), the NRC amended 10 CFR 
    50.59(b)(2) to reduce the regulatory burden on nuclear licensees. This 
    action revised the requirements for the annual submission of reports 
    for facility changes under 10 CFR 50.59. This action did not affect the 
    substance of the evaluation or the documentation required for 10 CFR 
    50.59 type changes. It only affected the interval for submission of the 
    information to the NRC. Instead of submitting the information annually, 
    the information can be submitted on a refueling cycle basis, provided 
    the interval between successive reports does not exceed 24 months.
        In order to take advantage of this reduction in regulatory burden, 
    the licensee has proposed an amendment to remove the submittal of a 
    report of facility changes under 10 CFR 50.59 from the Technical 
    Specification list of annual reporting requirements. Additionally, the 
    licensee has proposed corrections to minor administrative 
    inconsistencies in the TS Table of Contents and in a footnote 
    reference. The proposed changes are administrative only and do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated; or
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or
        3. Involve a significant reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location:  University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497
        NRC Project Director: Gail H. Marcus
    
    NOTICE OF ISSUANCE OF AMENDMENTS TO FACILITY OPERATING LICENSES
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station,Plymouth County, Massachusetts
    
        Date of application for amendment: May 1, 1996, as supplemented 
    August 12, 1996.
        Brief description of amendment: The amendment approves relocation 
    of the administrative controls related to the quality assurance review 
    and audit requirements of Section 6, Technical Specifications 6.5.B.8, 
    ``Nuclear Safety Review and Audit Committee-Audits,'' from the Pilgrim 
    Station Technical Specifications to the Boston Edison Quality Assurance 
    Manual (BEQAM). This change is in accordance with the guidance 
    contained in NRC Administrative Letter 95-06, ``Relocation of Technical 
    Specification Administrative Controls Related to Quality Assurance.'' 
    In addition, the Safety Evaluation includes the NRC staff review and 
    approval of the BEQAM changes in support of this amendment.
        Date of issuance: November 12, 1996
        Effective date: November 12, 1996
        Amendment No.: 168
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 5, 1996 (61 FR 
    28605) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 12, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of application for amendments: August 29, 1996, as 
    supplemented on September 20, 1996, and October 4, 1996.
        Brief description of amendments: The amendments change the 
    Technical Specifications to implement 10 CFR Part 50, Appendix J, 
    Option B, by referring to Regulatory Guide 1.163, ``Performance-Based 
    Containment Leakage-Test Program,'' with an exception as detailed in 
    the licensee's application.
        Date of issuance: November 12, 1996
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 175 and 162
    
    [[Page 64398]]
    
        Facility Operating License Nos. DPR-39 and DPR-48: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52964). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 12, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of application for amendment: August 14, 1996, as supplemented 
    October 18, 1996, and related application of January 18, 1996
        Brief description of amendment: The amendment revises the technical 
    specifications (TS) to allow one-cycle deferral of the inspection of 
    reactor coolant pump (RCP) flywheels.
        Date of issuance: November 7, 1996
        Effective date: November 7, 1996
        Amendment No.: 175
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 24, 1996 (61 
    FR 50054) The October 18, 1996, letter provided an updated TS page. 
    This change was within the scope of the original application and did 
    not change the staff's initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated November 7, 1996.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: December 14, 1994, as 
    supplemented by letters dated May 16 and August 29, 1996
        Brief description of amendments: The amendments will incorporate 
    guidance and recommendations for diesel generators contained in NUREG-
    1366, ``Improvements to Technical Specifications Surveillance 
    Requirements,'' Generic Letter (GL) 93-05, ``Line-Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operations,'' GL 94-01, ``Removal of Accelerated 
    Testing and Reporting Requirements for Emergency Diesel Generators,'' 
    and NUREG-1431, ``Revised Standard Technical Specifications for 
    Westinghouse PWRs.''
        Date of issuance: November 12, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 170 and 152
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 5, 1996 (61 FR 
    28612) The August 29, 1996, letter provided clarifying information that 
    did not change the scope of the December 14, 1996, application and the 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated November 12, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: August 1, 1996
        Brief description of amendment: The amendment revises the technical 
    specifications to incorporate requirements for limiting the time that 
    the hydrogen mixing isolation valves on the drywell are open. The 
    amendment also changes the time from 7 days to 31 days to determine the 
    cumulative time the valves are open.
        Date of issuance: November 12, 1996
        Effective date: November 12, 1996
        Amendment No.: 89
        Facility Operating License No. NPF-47. The amendment revised the 
    Technical Specifications/operating license.
        Date of initial notice in Federal Register: September 25, 1996 (61 
    FR 50343) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 12, 1996.No significant 
    hazards consideration comments received. No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
    
    Entergy Operations, Inc., System Energy Resources, Inc., 
    SouthMississippi Electric Power Association, and Entergy 
    Mississippi, Inc., Docket No. 50-416, Grand Gulf Nuclear Station, 
    Unit 1, Claiborne County, Mississippi
    
        Date of application for amendment: May 9, 1996, as supplemented by 
    letter dated August 27, 1996.
        Brief description of amendment: The amendment changed Surveillance 
    Requirements (SRs) 3.4.4.3, Safety/Relief Valves, 3.5.1.7, Automatic 
    Depressurization System Valves, and 3.6.1.6.1, Low-Low Set Valves, of 
    the Technical Specifications and allows the licensee to perform the 
    surveillance of the relief mode of operation of the safety/relief 
    valves on the main steam lines without physically lifting the disk of a 
    valve off the seat at power. The changes stated that the required 
    operation of the valve to verify is that the relief-mode actuator 
    strokes when the valve is manually actuated and the frequency of the 
    surveillances are in accordance with the inservice testing program for 
    the valves.
        Date of issuance: November 18, 1996
        Effective date: November 18, 1996
        Amendment No: 130
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47971) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 18, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: June 3, 1996, as supplemented 
    October 23, 1996
        Brief description of amendment: The amendment clarifies a 
    restriction on shutdown margin monitor operability while changing 
    operational modes, so that it only limits reactivity changes caused by 
    boron dilution and rod withdrawal. The amendment also corrects a 
    technical specification numerical reference so that the specification 
    number cited is in agreement with Amendment 99, dated December 29, 
    1994.
        Date of issuance: November 14, 1996
    
    [[Page 64399]]
    
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 131
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 20, 1996 (61 FR 
    31559) The October 23, 1996, letter provided clarifying information 
    that did not change the scope of the June 3, 1996, application and the 
    initial proposed no significant hazards consideration determination.The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated November 14, 1996No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: May 30, 1996
        Brief description of amendment: The proposed change to the 
    anticipated transient without scram recirculation pump trip logic for 
    the James A. Fitzpatrick Nuclear Power Plant allows for a high pressure 
    trip setpoint which is dependent upon the number of safety/relief 
    valves which are out of service.
        Date of issuance: November 7, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 237
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34896) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 7, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: May 30, 1996, as supplemented 
    October 17, and November 8, 1996
        Brief description of amendment: The proposed amendment changes the 
    FitzPatrick safety limit minimum critical power ratio from its current 
    value of 1.07 for two recirculation loop operation to 1.09 and from 
    1.08 to 1.10 for single recirculation loop operation for the Cycle 13 
    operation.
        Date of issuance: November 14, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 238
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34896) The October 17 and November 8, 1996 letters provided 
    supplemental information that did not change the initial no significant 
    hazards consideration determination.The Commission's related evaluation 
    of the amendment is contained in a Safety Evaluation dated November 14, 
    1996.No significant hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Southern Nuclear Operating Company, Inc., Docket No. 50-364, Joseph 
    M. Farley Nuclear Plant, Unit 2, Houston County, Alabama
    
        Date of amendment request: August 23, 1996, as supplemented by 
    letters dated September 16, November 6, 11 and 14, 1996
        Brief description of amendment: The amendment changes the Technical 
    Specifications (TS) to allow installation of laser welded elevated 
    tubesheet sleeves. Specifically, the amendment is for one cycle only 
    for Farley Unit 2. Permanent, generic TS changes for Westinghouse laser 
    welded sleeves for both units will be submitted prior to the next Unit 
    1 refueling outage currently scheduled for spring 1997.
        Date of issuance: November 20, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment No.: 117
        Facility Operating License No. NPF-8: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47982) The September 16, November 6, 11 and 14, 1996, letters 
    provided clarifying information that did not change the scope of the 
    August 23, 1996, application and the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated November 20, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: July 17, 1995.
        Brief description of amendments: These amendments revise the 
    frequency of surveillance requirements for certain plant protective 
    system instrumentation contained in Technical Specifications (TS) 
    3.3.1, ``Reactor Protective System (RPS) Instrumentation - Operating,'' 
    TS 3.3.2, ``Reactor Protective System (RPS) Instrumentation - 
    Shutdown,'' TS 3.3.3, ``Control Element Assembly Calculators (CEACs),'' 
    TS 3.3.4, ``Reactor Protective System (RPS) Logic and Trip 
    Initiation,'' TS 3.3.5, ``Engineered Safety Features Actuation System 
    (ESFAS) Instrumentation,'' and TS 3.3.6, ``Engineered Safety Features 
    Actuation System (ESFAS) Logic and Manual Trip.''
        Date of issuance: November 18, 1996
        Effective date: November 18, 1996, to be implemented within 30 days 
    of the date of issuance.
        Amendment Nos.: Unit 2 - 133 ; Unit 3 - 122
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45185) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 18, 1996.No significant 
    hazards consideration comments received: No.Temporary
        Local Public Document Room location:  Science Library, University 
    of California, P. O. Box 19557, Irvine, California 92713
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: September 4, 1996
        Brief description of amendment: This amendment revises Technical
    
    [[Page 64400]]
    
    Specification (TS) 6.2.3, ``Facility Staff Overtime,'' by removing 
    specific overtime limits and working hours and by adding procedural 
    controls to perform a monthly review of overtime hours.
        Date of issuance: November 8, 1996
        Effective date: November 8, 1996, to be implemented not later than 
    90 days after issuance
        Amendment No.: 212
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52970) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 8, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: July 18, 1996
        Brief description of amendment: The amendment adopts ASTM D-3803-
    1989 as the laboratory testing standard for charcoal samples from the 
    charcoal adsorbers in the auxiliary/fuel building emergency exhaust 
    system.
        Date of issuance: November 13, 1996
        Effective date: November 13, 1996, to be implemented within 30 days 
    of the date of issuance.
        Amendment No.: 118
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 14, 1996 (61 FR 
    42285) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 13, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Local Public Document Room location:  Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Dated at Rockville, Maryland, this 26th day of November 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II Office of Nuclear Reactor 
    Regulation
    [Doc. 96-30714 Filed 12-3-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Effective Date:
11/12/1996
Published:
12/04/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-21204
Dates:
November 12, 1996
Pages:
64381-64400 (20 pages)
PDF File:
x96-21204.pdf