X95-31206. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 60, Number 234 (Wednesday, December 6, 1995)]
    [Notices]
    [Pages 62485-62503]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X95-31206]
    
    
    
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    UNITED STATES NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from November 10, 1995, through November 24, 
    1995. The last biweekly notice was published on November 27, 1995 (60 
    FR 58395).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    
    [[Page 62486]]
        expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By January 5, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d). 
    
    [[Page 62487]]
    
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: May 2, 1995
        Description of amendments request: The proposed change revises the 
    large- break loss-of-coolant accident (LOCA) dose consequences. The 
    large-break LOCA dose calculation is being changed to include an 
    additional release path through allowable steam generator tube leakage 
    to the atmospheric dump valves (ADVs) or turbine bypass valves (TBVs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The probability or consequences of an accident previously 
    evaluated are not significantly increased by this change to the 
    large break LOCA dose consequences. This change has no effect on the 
    LOCA safety analysis for emergency core cooling system performance, 
    which demonstrates conformance to the acceptance criteria of 10 CFR 
    50.46, as described in the PVNGS Updated Final safety Analysis 
    Section 6.3.3. This change has no effect on structures, systems or 
    components prior to a LOCA or any other accident. The new 
    radiological consequences of the revised large break LOCA dose 
    calculation are below 10 CFR 100 limits for the exclusion area 
    boundary (EAB) and low population zone (LPZ), and the 10 CFR 50, 
    Appendix A, GDC 19 limits for the control room, as shown in Table 1-
    1, Column C. The NRC has previously approved changes to the PVNGS 
    LOCA dose consequences with the acceptance criteria that the doses 
    are still within the guidelines set forth in 10 CFR 100 and GDC 19. 
    This acceptance criteria is described in the Safety Evaluation 
    related to amendment Nos. 64, 50, and 37 to PVNGS Units 1, 2, and 3 
    respectively, dated September 8, 1992.
        The LOCA dose calculation is being changed to include an 
    additional release path through allowable steam generator tube 
    leakage to the ADVs or TBVs. This change is necessary to reflect a 
    revised calculation assumption that, following a large break LOCA, 
    the secondary system pressure would fall below reactor coolant 
    system pressure and containment pressure when operators cooldown the 
    steam generators by using ADVs or the TBVs (in accordance with the 
    safety analysis and EOPs [emergency operating procedures]). It is 
    desirable to use the ADVs or TBVs to vent secondary system steam and 
    thus reduce heat input to the reactor coolant system following a 
    large break LOCA. No other LOCA analysis assumptions are being 
    changed, and no changes are being made to structures, systems, 
    components or procedures.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This change has no impact on any structures, systems, 
    components, or procedures. The only impact is the revised 
    radiological consequences of a large break LOCA to include an 
    additional release path, as discussed in the response to Standard 1 
    above. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        This change to the large break LOCA dose consequences does not 
    involve a significant reduction in a margin of safety. The new 
    radiological consequences of the revised large break LOCA dose 
    calculation are below 10 CFR 100 limits for the EAB and LPZ, and the 
    10 CFR 50, Appendix A, GDC 19 limits for the control room, as 
    described in the response to Standard 1 above. The NRC has 
    previously approved changes to the PVNGS LOCA dose consequences with 
    the acceptance criteria that the doses are still within the 
    guidelines set forth in 10 CFR 100 and GDC 19. This acceptance 
    criteria is described in the Safety Evaluation related to amendment 
    Nos. 64, 50, and 37 to PVNGS Units 1, 2, and 3 respectively, dated 
    September 8, 1992. No equipment qualification is affected by the new 
    assumption of a release path through the secondary system following 
    a large break LOCA, and no post LOCA radiation zones will be 
    changed. This change has no impact on any structures, systems, 
    components, or procedures.
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: November 22, 1995
        Description of amendment request: The current Technical 
    Specifications (TS) Section 3.3.4.2 describes the limiting condition 
    during which components in the Service Water (SW) system may be 
    inoperable. The TS Section 3.3.4.2 states, in part, ``During power 
    operation, the requirements of 3.3.4.1 may be modified to allow any one 
    of the following components to be inoperable provided the remaining 
    systems are in continuous operation.'' The proposed change will delete 
    the qualifying statement,''... provided the remaining systems are in 
    continuous operation,'' from TS Section 3.3.4.2. Currently, this 
    statement requires the ``remaining systems to be in continuous 
    operation'' while allowing one SW loop header, or one SW pump, or one 
    SW booster pump to be inoperable for a period of 24 hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change would remove the requirement for the 
    remaining SW system components to be in continuous operation while 
    one TS-required component is inoperable. Rather, the remaining 
    components would remain operable, and no change would be made in 
    normal system operation. The SW system provides an accident 
    mitigation function and is not involved in accident initiation 
    sequences. Therefore, the proposed change would not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The capacity of the SW system is such that its accident 
    mitigation function can be performed by operation of a maximum of 
    two SW pumps, one SW booster pumps, and one SW header. While a TS-
    required component is inoperable, sufficient accident mitigation 
    capability is provided by the remaining operable components, rather 
    than requiring the remaining systems to be in continuous operation. 
    Therefore, the proposed change would not cause a significant 
    increase in the consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change would remove the requirement for the 
    remaining SW system 
    
    [[Page 62488]]
    components to be in continuous operation while one TS-required 
    component is inoperable. Rather, the remaining components would 
    remain operable. The proposed change would not change the normal 
    operation of the system, nor would any physical modifications result 
    from the change. The function and capability of the SW systems would 
    remain unchanged. Therefore, the proposed change would not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The proposed change would remove the requirement for the 
    remaining SW system components to be in continuous operation while 
    one allowed TS-required component is inoperable. Rather, the 
    remaining TS-required components would remain operable. Adequate 
    assurance of operability is maintained by performance of regular 
    surveillance testing. Maintaining operable status rather than 
    placing equipment in continuous operation does not result in a 
    change in the ability of the SW system to perform its intended 
    function, since the system provides an automatic response to 
    accident conditions, and the system possesses adequate capacity to 
    perform its normal operating function with one allowed TS-required 
    component inoperable. Therefore, the proposed change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: David B. Matthews
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: October 24, 1995
        Description of amendment request: The proposed amendment will 
    increase the trip setpoints and allowable values for the low power 
    block (P-7).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        In accordance with 10CFR50.92, CYAPCO has reviewed the proposed 
    change and has concluded that it does not involve a significant 
    hazards consideration (SHC). The basis for this conclusion is that 
    the three criteria of 10CFR50.92(c) are not compromised. The 
    proposed change does not involve an SHC because the change would 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change will relax the power level values for the P-
    7 interlock by 2 percent. This change affects both the P-7 and P-7N 
    interlocks. The P-7 interlock affects reactor trips on 1) low flow 
    in more than one reactor coolant loop, 2) reactor coolant pump bus 
    under voltage, 3) more than one reactor coolant pump breaker open, 
    4) main steam line isolation valve closure, 5) turbine trip, and 6) 
    variable low pressure. The P-7 interlock automatically blocks these 
    reactor trips on decreasing power and automatically unblocks these 
    reactor trips on increasing power. The P-7N interlock affects the 
    reactor trip on wide range, neutron flux, high startup rate. P-7N 
    automatically enables this reactor trip on decreasing power level 
    and automatically blocks this reactor trip on increasing power 
    level. The Applicable Modes requirement and Action Statements for 
    the P-7 interlock and the reactor trips associated with both P-7 and 
    P-7N in the Instrumentation Channel and Surveillance Requirements of 
    Technical Specification 3/4.3.1 are being changed by 2 percent to be 
    consistent with the change to P-7. The interlock setpoint cannot 
    cause an accident. Also, the proposed 2 percent increase in the 
    power level still results in a power level well below the power 
    level at which the P-7 interlocked reactor trips are required for 
    accident mitigation, as well as maintaining the high startup rate 
    trip enabled at a higher power level. This proposed power level is 
    consistent with the technical specification requirement prior to the 
    conversion to standard format technical specifications and is also 
    consistent with the Standard Westinghouse technical specification 
    value. Therefore, the proposed change can neither increase the 
    consequences of the design basis accident nor the probability of 
    occurrence of the design basis accidents.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed change only modifies the power level for the P-7 
    and P-7N interlocks. The proposed setpoint is a power level at which 
    stable plant conditions are easier to maintain while transferring 
    the power supply for the reactor coolant pumps between offsite power 
    and the main generator. The setpoint is also well below the power 
    level for which the reactor protection afforded by the trips that 
    are bypassed by P-7 is needed. This cannot create the possibility of 
    a new or different kind of accident from any previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        The proposed change maintains the power level for the P-7 
    interlock below the power level for which the reactor trips that are 
    blocked by the P-7 interlock are required. It also raises the power 
    level to a value at which it is easier to maintain stable plant 
    conditions. This will reduce the likelihood of an automatic reactor 
    trip during the transferring of power for the reactor coolant pumps 
    between offsite power and the main generator. The proposed change 
    will result in the high startup rate reactor trip being enabled at a 
    higher power level. This is conservative since it expands the range 
    of coverage for the trip. Therefore, the proposed change does not 
    impact the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: November 1, 1995
        Description of amendment request: The proposed amendment will 
    modifiy Surveillance Requirement 4.6.3.2, ``Containment Isolation 
    Valves,'' (CIVs) to change the surveillance interval from at least once 
    per 18 months to at least once per refueling interval.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        CYAPCO has reviewed the proposed change in accordance with 
    10CFR50.92 and concluded that the change does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    compromised. The proposed change does not involve an SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to Surveillance Requirement 4.6.3.2 of the 
    Haddam Neck Plant Technical Specifications extends the frequency for 
    verifying that each CIV actuates to its required position in 
    response to a safety injection actuation test signal. The proposal 
    would extend the frequency from at least once per 18 months to at 
    least once per 
    
    [[Page 62489]]
    refueling interval (24 months + 25% as allowed by Technical 
    Specification 4.0.2).
        The proposed change to Surveillance Requirement 4.6.3.2 does not 
    alter the intent or method by which the surveillance is conducted, 
    does not involve any physical changes to the plant, does not alter 
    the way any structure, system, or component functions, and does not 
    modify the manner in which the plant is operated.
        Additional assurance of CIV operability is provided by 
    Surveillance Requirement 4.6.3.3. Surveillance Requirement 4.6.3.3 
    requires the confirmation of the mechanical operability of the CIVs 
    by the inservice inspection program. The proposed change does not 
    modify these requirements.
        Equipment performance over the last four operating cycles was 
    evaluated to determine the impact of extending the frequency of 
    Surveillance Requirement 4.6.3.2. This evaluation included a review 
    of surveillance results, preventive maintenance records, and 
    corrective maintenance records. It has been concluded that the CIVs 
    are highly reliable, and that there is no indication that the 
    proposed extension could cause deterioration in valve condition or 
    performance.
        As such, the proposed change to the frequency of Surveillance 
    Requirement 4.6.3.2 will not degrade the ability of the CIVs to 
    perform their safety function.
        Based on the above, the proposed change to Surveillance 
    Requirement 4.6.3.2 of the Haddam Neck Plant Technical 
    Specifications does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed change to Surveillance Requirement 4.6.3.2 of the 
    Haddam Neck Plant Technical Specifications extends the frequency for 
    verifying that each CIV actuates to its required position in 
    response to a safety injection actuation test signal. The proposal 
    would extend the frequency from at least once per 18 months to at 
    least once per refueling interval (24 months + 25% as allowed by 
    Technical Specification 4.0.2).
        The proposed change does not alter the intent or method by which 
    the surveillance is conducted, does not involve any physical changes 
    to the plant, does not alter the way any structure, system, or 
    component functions, and does not modify the manner in which the 
    plant is operated. As such, the proposed change in the frequency of 
    Surveillance Requirement 4.6.3.2 will not degrade the ability of the 
    CIVs to perform their safety function.
        Based on the above, the proposed change to Surveillance 
    Requirement 4.6.3.2 of the Haddam Neck Plant Technical 
    Specifications will not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to Surveillance Requirement 4.6.3.2 of the 
    Haddam Neck Plant Technical Specifications extends the frequency for 
    verifying that each CIV actuates to its required position in 
    response to a safety injection actuation test signal. The proposal 
    would extend the frequency from at least once per 18 months to at 
    least once per refueling interval (24 months + 25% as allowed by 
    Technical Specification Section 4.0.2).
        The proposed change does not alter the intent or method by which 
    the surveillance is conducted, does not involve any physical changes 
    to the plant, does not alter the way any structure, system, or 
    component functions, and does not modify the manner in which the 
    plant is operated. As such, the proposed change in the frequency of 
    Surveillance Requirement 4.6.3.2 will not degrade the ability of the 
    CIVs to perform their safety function.
        Additional assurance of the operability of the CIVs is provided 
    by Surveillance Requirement 4.6.3.3.
        Equipment performance over the last four operating cycles was 
    evaluated to determine the impact of extending the frequency of 
    Surveillance Requirement 4.6.3.2. This evaluation included a review 
    of surveillance results, preventive maintenance records, and 
    corrective maintenance records. It has been concluded that the CIVs 
    are highly reliable, and that there is no indication that the 
    proposed extension could cause deterioration in valve condition or 
    performance.
        Based on the above, the proposed change to Surveillance 
    Requirement 4.6.3.2 of the Haddam Neck Plant Technical 
    Specifications does not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of amendment request: November 8, 1995, as supplemented 
    November 17, 1995
        Description of amendment request: The proposed amendment would 
    remove the prescriptive Type A containment leakage test rate frequency 
    of 40 plus or minus 10 months and add a reference to perform 
    containment leakage rate tests in accordance with the criteria 
    specified in Appendix J of 10 CFR Part 50 as amended by approved 
    exemptions. In addition, the proposed amendment would revise the test 
    pressure for Type B and C testing to correct a typographical error.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Leakage test rate frequency
        1) The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This change is administrative in nature and does not impact 
    plant systems, structures or components. The proposed change will 
    allow the facility's technical specifications to be revised to allow 
    containment sphere leakage testing in accordance with Appendix J to 
    10 CFR Part 50 as modified by approved exemptions.
        2) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This change is administrative in nature and does not impact 
    plant syst ems, structures or components. The proposed change will 
    allow the facility's technical specifications to be revised to allow 
    containment sphere leakage testing in accordance with Appendix J to 
    10 CFR Part 50 as modified by approved exemptions.
        3)The proposed change does not involve a significant reduction 
    in a margin of safety.
        This change is administrative in nature and does not impact 
    plant systems, structures or components. The underlying purpose of 
    Appendix J is still achieved. Appendix J states that the leakage 
    test requirements provide for periodic verification testing of the 
    leak tightness integrity of the primary reactor containment. The 
    appendix further states that the purpose of the tests is to assure 
    that leakage through the primary containment shall not exceed the 
    allowable leakage rate values as specified in the technical 
    specifications or associated bases. As stated previously, for Big 
    Rock Point and a large percentage of other plants, the Appendix J 
    Type B and C testing programs provide the most significant and 
    meaningful assessment of containment leak tightness. The testing 
    history and structural capability of the containment establish that 
    there is significant assurance that the extended interval between 
    Type A tests will not adversely impact the integrity of the 
    containment.
        Test pressure revision
        As stated in the technical specification change request, this 
    revision is being performed to be consistent with accident pressure, 
    Pa, used for Big Rock Point. 20 psig is a typographical error. 
    23 psig has always been used for these tests.
        The proposed change does not:
        1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        This change is administrative in nature and does not impact 
    plant systems, structures or components. The proposed change will 
    allow the facility's technical specifications to be revised to 
    reflect current containment sphere leakage testing in accordance 
    with Appendix J to 10 CFR Part 50. 
    
    [[Page 62490]]
    
        2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        This change is administrative in nature and does not impact 
    plant systems, structures or components. The proposed change will 
    allow the facility's technical specifications to be revised to 
    reflect current containment sphere leakage testing in accordance 
    with Appendix J to 10 CFR Part 50.
        3) involve a significant reduction in a margin of safety.
        This change is administrative in nature and does not impact 
    plant systems, structures or components.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201
        NRC Project Director: Brian E. Holian, Acting
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of amendment request: October 16, 1995
        Description of amendment request: Appendix J of 10 CFR Part 50, 
    ``Primary Reactor Containment Leakage Testing for Water-Cooled Power 
    Reactors,'' has recently been revised to include Option B. This option 
    allows the implementation of a performance based Type B and C testing 
    program. The proposed change will add a footnote to Technical 
    Specification (TS) 4.6.1.2.d stating that the Type B and C tests 
    scheduled for Unit 1 refueling outage Cycle 6 (1R6) will be conducted 
    in accordance with Option B and using the guidance of Regulatory Guide 
    1.163, Revision 0. This option is being incorporated into the 
    licensee's request to implement the improved TS. However, the improved 
    TS are not scheduled to become effective until after the Unit 1 
    refueling outage 1R6.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The change does not involve a significant increase in 
    probability or consequences of an accident previously evaluated. The 
    proposed change does not involve a change to structures, systems, or 
    components which would affect the probability or consequences of an 
    accident previously evaluated in the Vogtle Electric Generating 
    Plant (VEGP) Final Safety Analysis Report (FSAR). The proposed 
    change only provides a mechanism within the Technical Specifications 
    for implementing a performance-based method of determining the 
    frequency for leak rate testing which has been approved by the NRC 
    via a revision to 10 CFR 50, Appendix J.
        2. The proposed change will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed. 
    The amendment will not change the design, configuration, or method 
    of plant operation. It only allows for the implementation of Option 
    B of 10 CFR 50, Appendix J for Unit 1 refueling outage 1R6 without 
    violating the plant Technical Specifications.
        3. Operation of VEGP, Unit 1, in accordance with the proposed 
    change will not involve a significant reduction in the margin of 
    safety. The proposed change does not affect a safety limit, an LCO 
    [limiting condition for operation], or the way plant equipment is 
    operated. The NRC is aware that changes similar to this proposed 
    change are required in order to implement Option B of 10 CFR 50, 
    Appendix J. In fact, the staff indicates in Paragraph V.B. of 
    Appendix J that Option B or parts thereof may be adopted by a 
    licensee 30 days after the rule becomes effective by submitting 
    notification of its implementing plan and a request for revision to 
    Technical Specifications. Since the NRC has approved the provision 
    for performance-based testing and must approve this Technical 
    Specification[] change before the performance-based Option B can be 
    implemented, the margin of safety will not be significantly reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308
        NRC Project Director: Herbert N. Berkow
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: May 30, 1995 (noticed in the Federal 
    Register July 5, 1995, (60 FR 35080) as supplemented by letter dated 
    November 20, 1995
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications as follows:
        1. The Surveillance Frequency for the drywell bypass test is 
    changed from 18 months to 10 years with an increased testing frequency 
    required if performance degrades.
        2. The following changes are requested for the drywell air lock 
    testing: (a) the leakage rate surveillance is moved from the air lock 
    Limiting Condition for Operation (LCO) to the drywell LCO, (b) the 
    requirement for the air lock to meet a specific overall leakage limit 
    is deleted, (c) the Note that an inoperable air lock door does not 
    invalidate the previous air lock leakage test is deleted, (d) the Note 
    which required that the air lock leakage test at 3 psid be preceded by 
    pressurizing the air lock to 19.2 psid is moved to the bases, and (e) 
    the Surveillance Frequency for the air lock leakage test and interlock 
    test is changed from 18 months to 24 months.
        3. The Actions Notes in the drywell air lock LCO and the drywell 
    isolation valve LCO that identifies that the Actions required by the 
    drywell LCO must be taken when the drywell bypass leakage limit is not 
    met is deleted.
        4. The requirement for the drywell air lock seal leakage rate to 
    meet a specific leakage limit is deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration for River Bend Station (RBS) and Grand Gulf Nuclear 
    Station (GGNS), which is presented below:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The requested changes are either administrative changes which 
    clarify the format of the requirement or change the requirement to 
    match the design bases of the plant, a change which relocates the 
    requirement to the Technical Specification Bases, or a change in 
    surveillance interval. Each of these types of change are discussed 
    below:
        1. The administrative changes clarify the format of the 
    requirement or change therequirement to match the design bases of 
    the plant. Clarifying administrative format of 
    
    [[Page 62491]]
    the Technical Specifications does not result in any changes to the 
    Technical Specification requirements and, as a result, does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated. Also, changing the requirements of 
    the Technical Specifications to more closely match the design bases 
    of the plant will continue to assure that the plant will respond as 
    assumed in the accident analyses and, as a result, does not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed changes relocate information to the Technical 
    Specification Bases. In the Technical Specifications Bases the 
    relocated information will be maintained in accordance with 10 CFR 
    50.59 and subject to the change control provisions in Chapter 5 of 
    Technical Specifications. Since any changes to the Technical 
    Specifications Bases will be evaluated per the requirements of 10 
    CFR 50.59, no increase (significant or insignificant) in the 
    probability or consequences of an accident previously evaluated will 
    be allowed. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        3. The proposed changes in frequency for the drywell bypass 
    leakage and drywell air lock surveillances will continue to ensure 
    that no paths exist through passive drywell boundary components that 
    would permit gross leakage from the drywell to the primary 
    containment air space and result in bypassing the primary 
    containment pressure-suppression feature beyond the design basis 
    limit. The Mark III primary containment system satisfies General 
    Design Criterion 16 of Appendix A to 10 CFR Part 50. Maximum drywell 
    bypass leakage was determined previously by reviewing the full range 
    of postulated primary system break sizes. The limiting case was a 
    primary system small break loss of coolant accident (LOCA) and 
    yielded a design allowable drywell bypass leakage rate limit of 
    approximately 35,000 scfm for GGNS and 46,000 scfm (the Technical 
    Specification limit is based on a lower limit of 40,110 scfm) for 
    RBS. The Technical Specifications acceptable limit for the bypass 
    leakage following a surveillance is less than 10% of this design 
    basis value. The most recent bypass leakage value was approximately 
    2.5% for GGNS and .91% for RBS of the design allowable leakage rate 
    limit for the limiting event. EOI is committed to maintaining 
    programmatic and oversight controls that ensure that drywell bypass 
    leakage remains a small fraction of the design allowable leakage 
    limit.
        The drywell is typically exposed to essentially 0 psig during 
    normal plant operation and 3 psig during drywell bypass leak rate 
    testing. These pressures are considerably lower than the structural 
    integrity test pressure and are less likely to initiate a crack or 
    cause an existing crack to grow. Visual inspections of the 
    accessible drywell surfaces that have been performed since the 
    structural integrity tests have not revealed the presence of 
    additional cracking or other abnormalities. Therefore, additional 
    cracking of the drywell structure is not expected due to testing or 
    operation and, similar to the justification for the ten year 10 CFR 
    50 Appendix J Type A test interval, it is not considered credible 
    for the passive drywell structure to begin to leak sufficiently to 
    impact the design drywell bypass leakage limit.
        The primary containment's ability to perform its safety function 
    is fairly insensitive to the amount of drywell leakage, thereby 
    providing a margin to loss of the drywell safety function that is 
    not normally available for safety systems. This insensitivity is 
    demonstrated by the extremely high limiting event design basis 
    allowable leakage for the drywell (e.g., 35,000 scfm for GGNS and 
    46,000 scfm for RBS). The limiting leakage is almost an order of 
    magnitude higher for other events. Additionally, an even higher 
    allowable leakage can be realistically accommodated by the primary 
    containment due to the margins in the containment design. Because of 
    the margins available, it will take valves in multiple penetration 
    flow paths leaking excessively to cause the primary containment to 
    fail as a result of overpressurization, the probability that drywell 
    isolation valve leakage will result in primary containment failure 
    due to excessive drywell leakage is not considered significant and 
    this drywell/primary containment failure mode is not considered 
    credible.
        The proposed Technical Specification changes have no significant 
    impact on the GGNS Individual Plant Examination (IPE) or the RBS IPE 
    conducted per NRC Generic Letter 88-20. The IPEs considered 
    overpressurization failure of primary containment as part of the 
    primary containment performance assessment. Due to the magnitude of 
    acceptable drywell leakage and the extremely low probabilities of 
    achieving such leakage, primary containment failure due to 
    preexisting excessive drywell leakage was considered a non 
    significant contributor to primary containment failure. Primary 
    containment overpressurization failure can occur with or without 
    preexisting excessive drywell leakage in a severe accident. This is 
    due to physical phenomena associated with potentially extreme 
    environmental conditions inside primary containment following a 
    severe accident. However, the calculated frequency of such extreme 
    conditions is very small. The proposed changes do not impact the IPE 
    evaluated phenomena causing primary containment overpressurization 
    failure nor significantly increase the probability that the drywell 
    has preexisting excessive leakage and therefore would not contribute 
    to these accident scenarios.
        For the reasons discussed above, the proposed changes do not 
    have any significant risk impact to accidents previously evaluated 
    and do not significantly increase the consequences of an accident 
    previously evaluated. Additionally, drywell leakage is not the 
    initiator of any accident evaluated; therefore, changes in the 
    frequency of the surveillance for drywell leakage does not increase 
    the probability of any accident evaluated.
        Therefore, the proposed changes do not significantly increase 
    the probability or consequences of an accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The requested changes are either administrative changes which 
    clarify the format of the requirement or change the requirement to 
    match the design bases of the plant, a change which relocates the 
    requirement to the Technical Specification Bases, or a change in 
    surveillance interval. Each of these types of change are discussed 
    below:
        1. The administrative changes in the Technical Specification 
    requirements do not involve a physical alteration of the plant (no 
    new or different type of equipment will be installed) nor does it 
    change the methods governing normal plant operation. Thus, this 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        2. The proposed relocation of requirements does not involve a 
    physical alteration of the plant (no new or different type of 
    equipment will be installed) nor does it change the methods 
    governing normal plant operation. The proposed change will not 
    impose or eliminate any requirements. Adequate control of the 
    information will be maintained in the Technical Specification Bases. 
    Thus, the change proposed does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change modifies the surveillance frequency for 
    drywell bypass leakage and drywell air lock surveillances. The 
    changes only impact the test frequency and do not result in any 
    change in the response of the equipment to an accident. The changes 
    do not alter equipment design or capabilities. The changes do not 
    present any new or additional failure mechanisms. The drywell is 
    passive in nature and the surveillance will continue to verify that 
    its integrity has not deteriorated. Therefore, the proposed change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The requested changes are either administrative changes which 
    clarify the format of the requirement or change the requirement to 
    match the design bases of the plant, a change which relocates the 
    requirement to the Technical Specification Bases, or a change in 
    surveillance interval. Each of these types of changes are discussed 
    below:
        1. The administrative changes in the Technical Specification 
    requirements do not involve a physical alteration of the plant (no 
    new or different type of equipment will be installed) nor does it 
    change the methods governing normal plant operation. Thus, this 
    change does not cause a significant reduction in the margin of 
    safety. 
    
    [[Page 62492]]
    
        2. The relocation of requirements will not reduce a margin of 
    safety because it has no impact on any safety analysis assumptions. 
    In addition, the requirements to be transferred from the Technical 
    Specifications to the Technical Specifications Bases are the same as 
    the existing Technical Specifications. Since any future changes to 
    these requirements in the Technical Specifications Bases will be 
    evaluated per the requirements of 10 CFR 50.59, no reduction 
    (significant or insignificant) in a margin of safety will be 
    allowed.
        3. The proposed change modifies the surveillance frequency for 
    drywell bypass leakage and associated air lock surveillances. 
    Reliability of drywell integrity is evidenced by the measured 
    leakage rate during past drywell bypass leakage surveillances. 
    Appropriate design basis assumptions will be upheld, even when 
    combined with the complementary bypass leakage surveillances as 
    proposed. Drywell integrity will continue to be tested by means of 
    the proposed periodic drywell bypass leakage test, performance of 
    the drywell air lock door latching and interlock mechanism 
    surveillance, and performance of additional surveillances including 
    excercising of drywell isolation valves. The combination of these 
    surveillances will provide adequate assurance that drywell bypass 
    leakage will not exceed the design basis limit. Margins of safety 
    would not be reduced unless leakage rates exceeded the design 
    allowable drywell bypass leakage limit. Therefore, the proposed 
    change does not cause a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: October 26, 1995
        Description of amendment request: The proposed amendment would 
    revise the technical specifications for sixteen editorial changes and 
    would delete the requirement for a program to prevent and detect 
    Asiatic Clams (Corbicula) in the service water system (SWS). The 
    editorial changes covers such things as removing systems or components 
    that do not exist in the River Bend Station, correcting typographical 
    errors, correcting to be consistent with the writers guide for Improved 
    Technical Specifications, adding descriptions for systems to make them 
    clear, and wording changes to be consistent with approved facility 
    operations. The Corbicula program is no longer needed because the 
    facility has been modified and SWS no longer takes water from the 
    Mississippi River; source of the larvae and infestation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        EDITORIAL CHANGES
        The purposed changes involves reformatting, renumbering and 
    rewording of the existing Technical Specifications. The 
    reformatting, renumbering and rewording process involves no 
    technical changes to existing Technical Specifications. As such, 
    these changes are administrative in nature and do not impact 
    initiators of analyzed events or assumed mitigation of accident or 
    transient events. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed changes do not involve a physical alteration of the 
    plant (no new or different type of equipment will be installed) or 
    changes in methods governing normal plant operation. The proposed 
    changes will not impose or eliminate any new or different 
    requirements. Thus, these changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes will not reduce a margin of safety because 
    they have no impact on any safety analysis assumptions. These 
    changes are administrative in nature. As such, no question of safety 
    is involved, and the changes do not involve a significant reduction 
    in a margin of safety.
        CORBICULA PROGRAM
        The proposed change deletes the program associated with the 
    prevention and detection of Asiatic Clams (Corbicula) based upon 
    improvements to the non-safety related Normal Service Water System 
    (SWS). The source of makeup water to the SWS is no longer the 
    Mississippi River, which is the source of Asiatic Clams. 
    Demineralized water or well water is used eliminating the source of 
    asiatic clams. To prevent biofouling SWS is treated with chlorine/
    bromine. This program is not considered as an initiator for any 
    previously evaluated accident. Therefore, the proposed change will 
    not increase the probability or consequences of any accident 
    previously evaluated.
        The proposed change introduces no new mode of plant operation 
    and it does not involve a physical modification to the plant. The 
    possibility of the SES becoming contaminated by any other means is 
    highly unlikely since it is a ``closed-loop'' system. Therefore it 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Prevention of Asiatic Clam infestation in the SWS and associated 
    safety-related equipment is ensured by the ``closed-loop'' design of 
    the SWS. Post Refuel Outage (RF-4) inspections of the safety-related 
    heat exchangers that interface with the ``closed-loop'' SWS have 
    shown no evidence of clam infestations. Therefore, the change does 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: November 20, 1995
        Description of amendment request: The proposed amendment would 
    revise the technical specifications to eliminate the response time 
    testing requirements for selected Reactor Protection System 
    Instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The purpose of the proposed Technical Specification (TS) change 
    is to eliminate response time testing requirements for selected 
    components in the Reactor Protection System (RPS). The Boiling Water 
    reactors Owners' Group (BWROG) has completed an evaluating which 
    demonstrates that response time testing is redundant to the other 
    TS-required testing. These other tests, in conjunction with actions 
    taken in response to NRC Bulletin 90-01, ``Loss of Fill-Oil in 
    Transmitters Manufactured by Rosemount,'' and Supplement 1, are 
    sufficient to identify failure modes or degradation in instrument 
    response times and ensure operation of the associated systems within 
    acceptable limits. There are no known failure modes that can be 
    detected by response time testing that cannot also be detected by 
    the other TS-required testing. This evaluation was 
    
    [[Page 62493]]
    documented in NEDO-32291, ``System Analyses for Elimination of Selected 
    Response Time Testing Requirements,'' January 1994. Entergy 
    Operations, Inc. (EOI) has confirmed the applicability of this 
    evaluation to River Bend Station (RBS). In addition EOI will 
    complete the actions identified in the NRC staff's safety evaluation 
    of NEDO-32291.
        Because of the continued application of other existing TS-
    required tests such as channel calibration, channel checks, channel 
    functional tests, and logic system functional tests, the response 
    time of these systems will be maintained within the acceptance 
    limits assumed in plant safety analyses and required for successful 
    mitigation of an initiating event. The proposed changes do not 
    affect the capability of the associated systems to perform their 
    intended function within their required response time, nor do the 
    proposed changes themselves affect the operation of any equipment. 
    As a result, EOI has concluded that the proposed changes do not 
    involve a significant increase in the probability or the 
    consequences of an accident previously evaluated.
        The proposed changes only apply to the testing requirements for 
    the components identified above and do not result in any physical 
    change to these or other components or their operation. As a result, 
    no new failure modes are introduced. Therefore, the proposed changes 
    do not create the possibility of a new or different kind of accident 
    from any accidents previously evaluated.
        The current TS-required response times are based on the maximum 
    allowable values as assumed in the plant safety analyses. These 
    analyses conservatively establish the margin of safety. As described 
    above, the proposed changes do not affect the capability of the 
    associated systems to perform their intended function within the 
    allowed response time used as the basis for the plant safety 
    analyses. The potential failure modes for the components within the 
    scope of this request were evaluated for impact on instrument 
    response time. This evaluation confirmed that, with the exception of 
    loss of fill-oil of Rosemount transmitters, the remaining TS-
    required testing is sufficient to identify failure modes or 
    degradation in instrument response times and ensure operation of the 
    instrument within the scope of this request is within acceptable 
    limits. The actions taken in response to NRC Bulletin 90-09 and 
    Supplement 1 are adequate to identify loss of fill-oil failures of 
    Rosemount transmitters. As a result, it has been concluded that 
    plant and systems response to an initiating event will remain in 
    compliance with the assumptions of the safety analysis.
        Further, although not explicitly evaluated, the proposed changes 
    will provide an improvement to plant safety and operation by 
    reducing the time safety systems are unavailable, reducing the 
    potential for safety system actuations, reducing plant shutdown 
    risk, limiting radiation exposure to plant personnel, and 
    eliminating the diversion of key personnel resources to conduct 
    unnecessary testing. Therefore, EOI has concluded that this request 
    will result in an overall increase in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: September 22, 1995
        Description of amendment request: The proposed amendment would 
    modify a requirement of the Seabrook Station, Unit No. 1 Technical 
    Specifications. Specifically, the proposed amendment would change the 
    ACTION referenced in Table 3.3-3, Engineered Safety Features Actuation 
    System Instrumentation, for Functional Unit 8.b, Automatic Switchover 
    to Containment Sump/RWST Level Low-Low. The ACTION requirement would be 
    changed to ACTION 15 from ACTION 18. ACTION 15 requires an inoperable 
    channel to be placed in bypass (with no time limit specified) while 
    ACTION 18 requires an inoperable channel to be placed in the tripped 
    condition within 6 hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 
    CFR 50.92(c)(1)) because the proposed change would result in an 
    inoperable Functional Unit 8.b. protective channel being placed in 
    the bypassed condition vice tripped condition. Functional Unit 8.b. 
    is not involved in any accident initiation sequence; therefore, the 
    probability of a previously-analyzed accident is not increased. 
    Placing an inoperable Functional Unit 8.b. in bypass vice trip 
    reduces the probability of premature opening of the containment 
    building sump isolation valves thereby reducing the potential for 
    increasing the consequences of a previously-analyzed accident. Thus, 
    the consequences of a previously-analyzed accident is not increased.
        B. The change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    (10 CFR 50.92(c)(2)) because the change does not reduce the minimum 
    required number of channels of instrumentation to be operable. The 
    change does not alter the function of or affect the failure modes of 
    Functional Unit 8.b. instrumentation channels. The proposed change 
    does not otherwise affect the manner by which the facility is 
    operated, and it does not involve any changes to equipment or 
    features which affect the operational characteristics of the 
    facility.
        C. The change does not involve a significant reduction in a 
    margin of safety (10 CFR 50.92(c)(3)) because the change does not 
    reduce the minimum required number of channels of instrumentation to 
    be operable, and it does not involve any changes to equipment or 
    features which affect the operational characteristics of the 
    facility. Therefore, the protection previously provided remains 
    unchanged.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
        Attorney for licensee: Lillian M. Cuoco, Esquire, Northeast 
    Utilities Service Company, Post Office Box 270, Hartford CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London, 
    Connecticut
    
        Date of amendment request: May 26, 1995, supplemented and revised 
    October 20, 1995.
        Description of amendment request: The proposed changes would modify 
    TS 3.8.1.1., ``Electrical Power Systems, A.C. Sources, Operating,'' TS 
    3.8.1.2, ``Electrical Power Systems, Shutdown,'' TS 3.8.2.2, 
    ``Electrical Power Systems, A.C. Distribution - Shutdown,'' and TS 
    3.8.2.4, ``Electrical Power Systems, D.C. Distribution - Shutdown,'' to 
    provide operational flexibility as well as consistency between action 
    statements and to eliminate certain surveillance requirements that are 
    not applicable in Modes 5 or 6.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below: 
    
    [[Page 62494]]
    
        In accordance with 10 CFR 50.92, NNECO has reviewed the proposed 
    changes and has concluded that they do not involve an SHC. The basis 
    for this conclusion is that the three criteria of 10 CFR 50.92(c) 
    are not compromised. The proposed changes do not involve an SHC 
    because the change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to Surveillance Requirement 4.8.1.1.1 is 
    being made because presently, the surveillance requirement for 
    demonstrating offsite sources are operable states that ``two'' 
    independent circuits are required. The surveillance requirement is 
    referenced for both operating and shutdown modes. While it is 
    accurate for operating modes, it is inconsistent with the limiting 
    condition for operation for shutdown. The proposed change is safe 
    because it renders the surveillance requirement consistent with the 
    applicable limiting condition for operation (i.e., operating or 
    shutdown) and eliminates a potential source of confusion.
        The change to Surveillance Requirement 4.8.1.2 and Technical 
    Specification 3.8.2.2 merely clarifies the diesel generator 
    surveillance and operability requirements for Modes 5 and 6 and 
    renders action statements for related technical specification 
    sections consistent with and appropriate for operational Modes 5 and 
    6.
        Regarding diesel generator surveillance requirements, automatic 
    A.C. power for LNP events in Modes 5 and 6 is not required. This is 
    validated by the fact that the undervoltage sensors are only 
    required to be operable in Modes 1, 2 and 3 to meet technical 
    specifications. Because the undervoltage sensors provide the logic 
    that results in actuation of the sequencer, it follows that the 
    sequencer need not be operable in Modes 5 and 6. Accordingly, the 
    sequencer is not required to support operability of the available 
    diesel generator in Modes 5 and 6. Further, because SIAS is blocked 
    in Modes 5 and 6, automatic start of the diesel generator upon 
    receipt of a SIAS is similarly not required to support operability 
    of the diesel generator in Modes 5 and 6.
        Additionally, operation of the diesel generator in parallel with 
    the system during Modes 5 and 6 is not required to perform its 
    intended safety function. In fact, such operation may compromise 
    both sources as the result of a single event.
        Since automatic A.C. power is not credited in the mitigation of 
    Mode 5 and 6 events and accidents, such as fuel handling accidents, 
    there is no increase in the probability or consequences of 
    previously evaluated accidents.
        The action statement in Technical Specification 3.8.2.2 has been 
    revised to cite actions that are more appropriate for Modes 5 and 6 
    for Millstone Unit No. 2. This is due to the ability to maintain the 
    plant in a safe condition without needing to automatically load the 
    diesel generator through the sequencers in Modes 5 and 6. In 
    addition, the proposed change is consistent with the CE Owner's 
    Group Standard Technical Specification and with other Millstone Unit 
    No. 2 action statements. Consequently, there is no increase in the 
    probability or consequences of previously evaluated accidents.
        The change to TS 3.8.2.4 merely renders the action statement 
    consistent with, and appropriate for, operational Modes 5 and 6.
        Since D.C. power is not credited in the mitigation of Mode 5 and 
    6 events and accidents, such as fuel handling accidents, there is no 
    increase in the probability or consequences of previously evaluated 
    accidents.
        The action statement in TS 3.8.2.4 has been revised to cite 
    actions that are more appropriate for Modes 5 and 6 for Millstone 
    Unit No. 2. This is due to the ability to maintain the plant in a 
    safe condition without D.C. power distribution available in Modes 5 
    and 6. In addition, the proposed change is consistent with the CE 
    Owner's Group Standard Technical
        Specifications (NUREG-1432) and with other Millstone Unit No. 2 
    action statements. Consequently, there is no increase in the 
    probability or consequences of previously evaluated accidents.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed changes do not alter or affect the design, 
    function, failure mode, or operation of the plant. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to the technical specifications provides 
    greater consistency between the action statements and clarifies 
    which surveillance requirements are required in Modes 5 and 6. Since 
    the diesel generators are not required to be loaded automatically in 
    Modes 5 and 6, and since it is part of our shutdown risk management 
    program to assure that adequate cooling is able to be provided, and 
    since the diesel will still be verified to start and achieve rated 
    speed, the proposed changes to the technical specifications do not 
    reduce the margin of safety.
        The proposed change to the TS provides greater consistency among 
    action statements during Modes 5 and 6. Since the D.C. distribution 
    system is not credited in the mitigation of Mode 5 and 6 events and 
    accidents, and since it is part of our shutdown risk management 
    program to assure that adequate fuel cooling is able to be provided, 
    the proposed change to the TS does not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: June 27, 1995, as supplemented July 21, 
    1995
        Description of amendment request: The amendment revises the 
    Technical Specifications (TS) to relocate TS requirements for the 
    containment purge exhaust and supply valves, and to remove a duplicate 
    testing requirement for the safety injection input from engineered 
    safety features from the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ... The proposed changes do not involve an SHC [significant 
    hazards consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The first proposed change relocates the operability and 
    surveillance requirements for the containment high range radiation 
    monitors from Technical Specification Section 3.3.3 to Technical 
    Specification Section 3.3.2. The proposed changes are administrative 
    in nature. The proposed changes do not alter the way any structure, 
    system, or component functions and do not modify the manner in which 
    the plant is operated and do not involve any physical changes to the 
    plant.
        The second proposed modification will delete the testing 
    requirement for functional unit 16, ``Safety Injection Input from 
    ESF,'' of Table 4.3-1 because the logic circuitry that processes
        the safety injection signals and produces a reactor trip is 
    tested under functional unit 19 ``Automatic Trip and Interlock 
    Logic,'' and the testing is performed on a more frequent basis 
    (i.e., on a monthly staggered bases versus on an 18-month 
    frequency). In addition, the same logic testing is accomplished with 
    an 18-month TADOT of functional unit 1.a of Table 4.3-2 and with a 
    monthly staggered actuation logic testing of functional unit 16 of 
    Table 4.3-2. This testing ensures that operability of the logic 
    under functional unit 16 of Table 4.3-1 is verified. The other tests 
    will continue to verify the operability of the reactor trip system 
    and that a reactor trip will be initiated when required.
        Therefore, there is no change in the potential for an increase 
    in the consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed. 
    
    [[Page 62495]]
    
        The proposed changes do not affect the operation or response of 
    any plant equipment or introduce any new failure mechanisms. The 
    proposed elimination of the testing requirement line item does not 
    affect the test results since the logic circuitry that processes the 
    safety injection signal and produces a reactor trip will be tested 
    and is tested under functional unit 19 of Table 4.3-1. As such, the 
    changes do not create the possibility of a new or different kind of 
    accident previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The proposed changes do not have any adverse impact on the 
    protective boundaries nor do they affect the consequences of any 
    accident analyzed. The operability and surveillance requirements, 
    although relocated to other technical specifications, will still 
    ensure that the system (the radiation monitors) is tested and within 
    limits. The proposed elimination of the testing equipment will not 
    change the performance or operating conditions of the safety 
    systems. The operable reactor trip system instrumentation ensures 
    that the assumptions in the Bases of the Technical Specifications 
    are not affected and ensures that the margin of safety is not 
    reduced. Therefore, the proposed changes do not reduce the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: November 14, 1994
        Description of amendment requests: The proposed amendment would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Nuclear Power Plant, Unit Nos. 1 and 2, for the slave relay test 
    frequency from quarterly (Q) to refueling (R). The request would also 
    remove table notation 4 from Table 4.3-2. The associated Bases would 
    also be appropriately revised.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The results of WCAPs 14117 and 13878 demonstrate that slave 
    relays are highly reliable. The WCAPs also provide guidance to 
    assure that slave relays remain highly reliable. The aging 
    assessment concludes that the age/temperature-related degradation of 
    all ND relays, and NE relays produced after May 1990, is 
    sufficiently slow such that a refueling frequency surveillance 
    interval will not significantly increase the probability of slave 
    relay failures. Finally, the evaluation of the interposing slave 
    relays in the emergency diesel generator start circuitry, control 
    room ventilation and auxiliary building ventilation realignments, 
    steam generator blowdown isolation and radwaste isolation systems 
    has concluded that based on the tests of the interposing relays 
    performed during other equipment testing, reasonable assurance is 
    provided that failures will be identified if the associated slave 
    relays are tested on a refueling frequency.
        The removal of table notation 4 from TS Table 4.3-2 is an 
    administrative change that eliminates unnecessary redundancy from 
    the TS and does not affect plant operation.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not alter the performance of the ESFAS 
    mitigation systems assumed in the plant safety analysis. Changing 
    the interval for periodically verifying ESFAS slave relays (assuring 
    equipment operability) will not create any new accident initiators 
    or scenarios.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated for DCPP.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect the total ESFAS response 
    assumed in the safety analysis since the reliability of the slave 
    relays will not be significantly affected by the increased 
    surveillance frequency.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: August 18, 1995, as supplemented on 
    November 1, 1995
        Description of amendment request: The proposed amendment would 
    revise the Operating License and Technical Specifications to allow for 
    a power uprate to 2900 MWt. The current maximum power level is 2775 
    MWt.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
        Implementation of uprate power operation does not contribute to 
    any accident evaluated in the FSAR [Final Safety Analysis Report]. 
    The NSSS [Nuclear Steam Supply System] Components (RV [reactor 
    vessel], RCPs [reactor coolant pumps], CRDMs [control rod drive 
    mechanisms], SGs [steam generators], and piping) are compatible with 
    the revised operating conditions. These components have been 
    reanalyzed and the results show that ASME [American Society of 
    Mechanical Engineers] Code requirements remain satisfied and are 
    within the current Licensing Basis.
        Interfacing Systems which are important to safety are not 
    adversely impacted and will continue to perform their design 
    function. Overall secondary plant performance is not significantly 
    altered by the proposed changes.
        The revision to the Pressure Temperature Limits will not 
    adversely impact the RCS [reactor coolant system] Pressure Boundary. 
    The length of time these curves will be applicable, due to increased 
    neutron fluence, is being reduced. Before the 13 Effective Full 
    Power Years have elapsed, new curves will be generated to reflect 
    the analysis of the specimen capsule and will be derived utilizing 
    NRC approved methodology.
        Therefore, since the Reactor Coolant pressure boundary integrity 
    and system functions are not adversely impacted, the probability of 
    occurrence of an accident evaluated in the VCSNS [Virgil C. Summer 
    Nuclear Station] FSAR will be no greater than the original design 
    basis of the plant.
        An extensive analysis has been performed to evaluate the 
    consequences of the following accident types currently evaluated in 
    the VCSNS FSAR: 
    
    [[Page 62496]]
    
        - Non-LOCA [loss-of-coolant accident] Events
        - Large Break and Small Break LOCA
        - Steam Generator Tube Rupture
        With the [delta]75 SGs and revised operating conditions, the 
    calculated results (i.e., DNBR [departure from nucleate boiling 
    ratio], Primary and Secondary System Pressure, Peak Clad 
    Temperature, Metal Water Reaction, Challenge to Long Term Cooling, 
    Environmental Conditions Inside and Outside containment, etc.) for 
    the accidents are similar to those currently reported in the VCSNS 
    FSAR and remain within applicable Regulatory Acceptance Criteria. 
    Select results (i.e., Containment Pressure during a Steam Line 
    Break, Minimum DNBR for Rod Withdrawal from Subcritical, etc.) are 
    slightly more limiting than those currently reported in the FSAR due 
    to the use of the assumed operating conditions with the [delta]75 
    SGs and in some cases, use of an uprated core power of 2900 MWt. 
    However, in all cases, the calculated results do not challenge the 
    integrity of the primary/secondary/ containment pressure boundary 
    and remain within the regulatory acceptance criteria applied to 
    VCSNS's current licensing basis.
        Given that calculated radiological consequences are not 
    significantly higher than current FSAR results and remain well 
    within 10 CFR 100 limits, it is concluded that the consequences of 
    an accident previously evaluated in the FSAR are not significantly 
    increased.
        2. The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Uprate power operation will not introduce any new accident 
    initiator mechanisms. Structural integrity of the RCS is maintained 
    during all plant conditions through compliance with the ASME code 
    and 10 CFR 50 Appendix G requirements. Design requirements of 
    auxiliary systems are met with the RSGs [replacement steam 
    generators] and uprate power operation. No new failure modes or 
    limiting single failures have been identified. Since the safety and 
    design requirements continue to be met and the integrity of the 
    reactor coolant system pressure boundary is not challenged, no new 
    accident scenarios have been created. Therefore, the types of 
    accidents defined in the FSAR continue to represent the credible 
    spectrum of events to be analyzed which determine safe plant 
    operation.
        3. The proposed license amendment does not involve a significant 
    reduction in a margin of safety.
        Although uprate power operation will require changes to the 
    VCSNS Technical Specifications, the proposed changes are supported 
    by extensive LOCA, NON-LOCA and SGTR [steam generator tube rupture] 
    analyses. These analyses show acceptable consequences with margin to 
    the applicable regulatory limits. All equipment required to function 
    during accident conditions has been shown to remain qualified and 
    thus will perform their design function, and all components remain 
    in compliance with the codes and standards in effect when VCSNS was 
    originally licensed (with the exception of the replacement steam 
    generators which use the 1986 ASME Code Section III Edition).
        Low Temperature Overpressure transients which could challenge 
    RCS structural integrity are not impacted by the revision to the 
    Pressure Temperature Limitations Curves. The curves are not directly 
    impacted, the changes do not reduce any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: Frederick J. Hebdon
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: August 29, 1995
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications for allowable values and trip 
    setpoints for selected plant process instrumentation. The new allowable 
    values/setpoints are in accordance with the instrument setpoint 
    methodology accepted by the NRC staff in a letter dated July 18, 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed revised Trip Setpoints and Allowable Values are 
    more conservative than those currently approved in the Technical 
    Specifications. Therefore, any proposed system or component 
    actuations will occur earlier, resulting in a more conservative 
    plant response. Thus, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change to the Technical Specifications does not 
    introduce any new components nor does it modify the design of any 
    existing components. Other than making Trip Setpoints and Allowable 
    Values of existing instrumentation more conservative, the change 
    does not affect the design or function of any plant system, 
    structure, or component, nor does it change the way plant systems 
    are operated. Thus, the possibility of a new or different kind of 
    accident previously evaluated is not created.
        3. The proposed change does not result in a significant 
    reduction in the margin of safety.
        Since the proposed revised Trip Setpoints and Allowable Values 
    are more conservative than the existing values, the margin of safety 
    would be increased by issuance of the changes. Thus, the proposed 
    change does not result in a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: November 2, 1995
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to allow 120 volt AC buses EV-1-A 
    and EV-1-B to be energized from either their normal inverter power 
    supply or from their alternate power supply.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated:
        These buses are not used as the initiator of any analyzed 
    accidents. Therefore, the probability of any previously evaluated 
    accident has not increased. If an accident were to occur while the 
    buses are supplied from the alternate power supply, there would 
    
    [[Page 62497]]
    be no change in the analyzed accident scenario since even in the event 
    of a loss of offsite power event, the safety functions would be 
    completed. Thus, the consequences of any previously evaluated 
    accident have not increased.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated:
        The proposed change introduces no new mode of plant operation 
    and it does not involve physical modification to the plant. 
    Therefore, it does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety:
        This change does not involve a significant reduction in a margin 
    of safety since the proposed change maintains a safety related, 
    diesel-backed power supply to these buses whether the power is 
    supplied from the inverters or from the alternate power supply. If a 
    loss of offsite power event were to occur while the buses were 
    supplied from the alternate power source, the safety functions being 
    performed by components supplied from these buses would occur. Thus, 
    there has been no reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: November 2, 1995
        Description of amendment request: The proposed amendment to the 
    Perry Nuclear Power Plant Technical Specifications revises those 
    specifications associated with handling irradiated fuel in Primary 
    Containment and the Fuel Handling Building, and selected specifications 
    associated with CORE ALTERATIONS. Specifically, analysis identifies 
    that only recently irradiated fuel contains sufficient fission 
    products to require OPERABILITY of accident mitigation features to meet 
    the accident analysis assumptions. Analyses also show that accident 
    mitigation features such as building INTEGRITY and engineered safety 
    feature (ESF) ventilation systems are not required for CORE ALTERATION 
    events.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
         The proposed requirements are imposed during specific 
    activities which can be postulated to result in significant 
    radioactive releases. The proposed APPLICABILITY requirements are 
    consistent with either the original design basis analyses or with 
    revised analyses performed to support this proposed amendment. 
    Because the equipment controlled by the revised Specifications is 
    not considered an initiator to any previously analyzed accident, 
    inoperability of the equipment cannot increase the probability of 
    any previously evaluated accident.
        Consistent with the original design basis analysis, the reanalysis 
    concludes that radiological consequences of the fuel handling accident 
    are well within the 10 CFR 100.11 limits, as defined by acceptance 
    criteria in Standard Review Plan Section 15.7.4. The reanalysis has 
    previously been submitted to the Nuclear Regulatory Commission for 
    review, and NRC confirmatory calculations reached consistent results 
    (reference NRC Safety Evaluation for License Amendment No. 35). The 
    results of the CORE ALTERATION events other than the fuel handling 
    accident remain unchanged from the original design basis, which showed 
    that these events do not result in fuel cladding integrity damage or 
    radioactive releases. Therefore, the proposed changes do not 
    significantly increase the consequences of any previously evaluated 
    accident.
        Based on the above, the proposed changes do not significantly 
    increase the probability or consequences of any accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed requirements are imposed when specific activities 
    represent situations where significant radioactive releases can be 
    postulated. The proposed APPLICABILITY requirements are consistent 
    with design basis analyses. The proposed changes do not introduce 
    any new modes of plant operation and do not involve physical 
    modifications to the plant. Therefore, the proposed changes do not 
    create the possibility of a new or different kind of accidident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
         The proposed change imposes controls to ensure that during 
    performance of activities which represent situations where 
    radioactive releases are postulated, the radiological consequences 
    are at or below the established licensing limit. Safety margins and 
    analytical conservatisms have been evaluated and are well 
    understood. Substantial conservatism is retained to ensure that the 
    analysis adequately bounds all postulated event scenarios. The 
    current margin of safety is retained.
         Specifically, the margin of safety for the fuel handling 
    accident is the difference between the 10 CFR 100 limits and the 
    licensing limit defined by the Standard Review Plan (NUREG 0800), 
    Section 15.7.4. The licensing limit is defined by the Standard 
    Review Plan as being well within the 10 CFR 100 limits, with 
    ``well within'' defined as 25% of the 10 CFR 100 limits for the fuel 
    handling accident. Excess margin is the difference between the 
    postulated doses and the corresponding licensing limit. In the NRCs 
    initial licensing review of the Perry Nuclear Power Plant (NUREG-
    0887, Section 15.3.3), the NRC accepted the design and analyses 
    based on the results of the analyses being well within the guideline 
    values of 10 CFR 100.
        The proposed APPLICABILITY requirements continue to ensure that 
    the whole-body and thyroid doses at the exclusion area and low 
    population zone boundaries as well as control room doses are at or 
    below the corresponding licensing limit. The margin of safety is 
    unchanged; therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The margin of safety for the CORE ALTERATION events other than 
    the fuel handling accident discussed above also remains the same as 
    in the original design basis analyses, since the proposed changes do 
    not impact on the Technical Specification requirements for systems 
    needed to prevent or mitigate such CORE ALTERATION events.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and 
    
    [[Page 62498]]
    requirements of the Atomic Energy Act of 1954, as amended (the Act), 
    and the Commission's rules and regulations. The Commission has made 
    appropriate findings as required by the Act and the Commission's rules 
    and regulations in 10 CFR Chapter I, which are set forth in the license 
    amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of application for amendments: October 6, 1995, and 
    supplemented November 20, 1995
        Brief description of amendments: The amendments revise the 
    Technical Specifications by incorporating a new acceptance criterion 
    for steam generator tubes with degradation in the tubesheet roll 
    expansion region.
        Date of issuance: November 21, 1995
        Effective date: November 21, 1995
        Amendment Nos.: 172 and 159
        Facility Operating License Nos. DPR-39 and DPR-48: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 16, 1995 (60 FR 
    53648) The supplemental letter provided clarifying information that did 
    not affect the initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 21, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of application for amendment: August 10, 1995
        Brief description of amendment: The amendment revises the Haddam 
    Neck Technical Specification Section 3/4.4.3, ``Pressurizer,'' to add a 
    footnote to allow the pressurizer level to be controlled, outside of 
    the programmed level, between 25 to 50 percent, plus or minus 5 percent 
    in Mode 3 when the reactor coolant system is borated to the required 
    Mode 5 concentrations.
        Date of Issuance: November 14, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 186
        Facility Operating License No. DPR-61. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52928) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated November 14, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: September 13, 1995, as 
    supplemented October 16,1995
        Brief description of amendments: These amendments revise the 
    Administrative Controls section of the BVPS-1 and BVPS-2 TSs to make 
    them consistent with the requirements of the Offsite Dose Calculation 
    Manual (ODCM). The ODCM was recently updated to reflect the radioactive 
    liquid and gaseous effluent release limits and the liquid holdup tank 
    activity limit of BVPS-1 License Amendment No. 188 and BVPS-2 License 
    Amendment No. 70 which were issued June 12, 1995.
        Date of issuance: November 21, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 10 days.
        Amendment Nos.: 194 and 77
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 22, 1995 (60 
    FR 49292) The October 16, 1995, letter did not change the initial 
    proposed no significant hazards consideration determination or expand 
    the amendment request beyond the scope of the September 22, 1995, 
    Federal Register notice. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated November 21, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: February 14, 1994, as supplemented by 
    letters dated July 25, August 15, and August 29, 1995
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications (TSs) to make them consistent with the 
    revised 10 CFR Part 20, Standards for Protection Against Radiation.
        Date of issuance: November 17, 1995
        Effective date: November 17, 1995
        Amendment No.: 116
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14888) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 17, 1995. The July 25, 
    August 15, and August 29, 1995 letters provided clarifying information 
    that did not change the initial propose no significance hazards 
    consideration determination.
        No significant hazards consideration comments received: No
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: May 12, 1995, as supplemented 
    by letters dated July 6 and October 2, 1995. 
    
    [[Page 62499]]
    
        Brief description of amendments: The amendments revise Technical 
    Specification Surveillance Requirement 4.6.1.2 to add the provision 
    that 10 CFR Part 50, Appendix J, applies, except as modified by NRC-
    approved exemptions.
        Date of issuance: November 17, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 91 and 69
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35078) The July 6 and October 2, 1995, letters provided clarifying 
    information that did not change the scope of the May 12, 1995, 
    application and initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 17, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: July 28, 1995, as supplemented 
    September 12, October 18, and October 31, 1995.
        Brief description of amendment: In order to support a full-core 
    offload as a normal end-of-cycle event, the amendment adds License 
    Condition 2.C(6) and will require that: (1) the reactor be subcritical 
    for at least 100 hours prior to the start of reactor refueling 
    operations, (2) the spent fuel pool bulk temperature be maintained less 
    than or equal to 140F, and (3) two trains of shutdown cooling be 
    operable during reactor refueling operations.
        Date of issuance: November 9, 1995
        Effective date: As of the date of issuance.
        Amendment No.: 89
        Facility Operating License No. DPR-21. Amendment revised the 
    license.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45180) The September 12, October 18, and October 31, 1995, submittals 
    provided additional information that did not change the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment and Final No 
    Significant Hazards Consideration Determination are contained in a 
    Safety Evaluation dated November 9, 1995.
        No significant hazards consideration comments received: No public 
    comments received. A request for a hearing was received from We the 
    People, the Seacoast Anti-Pollution League, the New England Coalition 
    on Nuclear Pollution, and Donald Del Core of Uncasville, Connecticut.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: October 6, 1995, supplemented 
    October 23, November 2, and November 15, 1995.
        Brief description of amendment: The amendment adds footnotes to 
    Action Statement (AS) 3.8.1.1.a of the Technical Specification (TS) and 
    its bases to allow a one-time extension of the allowed outage time 
    (AOT) for an inoperable offsite power source from the current 72 hours 
    to 7 days.
        Date of issuance: November 22, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.:  192
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 17, 1995 (60 FR 
    53812). The October 23, November 2, and November 15, 1995, letters 
    provided clarifying information and slight modifications to the 
    original request that were not outside the scope of the original notice 
    and did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated November 22, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location:  Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360
    
    Northern States Power Company, Docket No. 50-282, Prairie Island 
    Nuclear Generating Plant, Unit No. 1, Goodhue County, Minnesota
    
        Date of application for amendment: January 10, 1995, as 
    supplemented August 9 and September 20, 1995.
        Brief description of amendment: The amendments revise the Prairie 
    Island event monitoring instrumentation Technical Specifications and 
    associated Bases to conform to Standard Technical Specifications for 
    post-accident monitoring.
        Date of issuance: November 9, 1995
        Effective date: November 9, 1995, with full implementation within 
    30 days.
        Amendment Nos.: 121/114
        Facility Operating License No. DPR-42 and DPR-60. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8753) The August 9 and September 20, 1995, letters provided updated 
    Technical Specification pages and clarifying information in response to 
    discussions with the staff during various teleconferences conducted 
    during the review process. This information was within the scope of the 
    original application and did not change the staff's initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated November 9, 1995.
        No Significant hazards consideration comments received: No
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: December 2, 1994, as 
    supplemented May 12, 1995.
        Brief description of amendments: These amendments relocate the fire 
    protection requirements from the Technical Specifications to the 
    Updated Final Safety Analysis Report in accordance with the guidance in 
    Generic Letter (GL) 86-10, ``Implementation of Fire Protection 
    Requirements,'' and GL 88-12, ``Removal of Fire Protection Requirements 
    from Technical Specifications.''
        Date of issuance: November 20, 1995 Effective date: As of date of 
    issuance, both units, to be implemented within 30 days.
        Amendment Nos.: 104 and 68
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications and the License.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20524) The supplemental letter provided clarifying information and did 
    not 
    
    [[Page 62500]]
    change the initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 20, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: September 14, 1995 and 
    supplemented by letter dated October 27, 1995
        Brief description of amendments: These amendments revise the 
    technical specifications by deleting Reactor Enclosure and Refueling 
    Area Secondary Containment Isolation Valve Tables 3.6.5.2.1-1 and 
    3.6.5.2.2-1, and references to them, in accordance with Generic Letter 
    91-08, ``Removal of Component lists from Technical Specifications.'' 
    The TS have been modified to state requirements in general terms that 
    include the components listed in the tables removed from the TS.
        Date of issuance: November 20, 1995
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment Nos.: November 20, 1995
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52934) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 20, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464
    
    Tennessee Valley Authority, Docket No. 50-296, Browns Ferry Nuclear 
    Plant, Unit 3, Limestone County, Alabama
    
        Date of application for amendments: October 4, 1995 (TS 368)
        Brief description of amendment: The amendment delete requirements 
    for daily checks for certain instruments that do not have indications, 
    and provides editorial changes.
        Date of issuance: November 13, 1995
        Effective Date: November 13, 1995
        Amendment No.: 202
        Facility Operating License No. DPR-68: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52935) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 13, 1995.
        No significant hazards consideration comments received: None
        Local Public Document Room location:  Athens Public library, South 
    Street, Athens, Alabama 35611
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: August 7, 1995 (TS 95-03)
        Brief description of amendments: The amendments address operation 
    with a rod urgent failure condition, including limited operation with 
    one control or shutdown bank inserted up to 18 steps below its 
    insertion point. In addition, the surveillance interval for rod 
    movement verifications has been increased from 31 to 92 days.
        Date of issuance: November 21, 1995
        Effective date: November 21, 1995
        Amendment Nos.: 215 and 205
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45186) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 21, 1995.
        No significant hazards consideration comments received: None
        Local Public Document Room location:  Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: April 28, 1995
        Brief description of amendment: The amendment removes the license 
    conditions for the Transamerica Delaval, Inc. emergency diesel 
    generators specified by paragraph 2.C.(9) and defined in Attachment 2 
    to the Operating License.
        Date of issuance: November 16, 1995
        Effective date: November 16, 1995
        Amendment No.: 74
        Facility Operating License No. NPF-58: This amendment revises the 
    license.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29889) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 16, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: June 23, 1995, and facsimile 
    transmission dated October 31, 1995
        Brief description of amendment: This amendment relocates TS 3/
    4.3.3.3, ``Seismic Instrumentation;'' TS 3/4.3.3.4, ``Meteorological 
    Instrumentation;'' and TS 3/4.4.11, ``Reactor Coolant System Vents;'' 
    and the Bases for each of the three sections from the TS to the Updated 
    Safety Analysis Report, and eliminates the special reporting 
    requirements for inoperable seismic and meteorological monitoring 
    instrumentation from TS 6.9.2.
        Date of issuance: November 14, 1995 Effective date: November 14, 
    1995, and shall be implemented not later than 90 days after issuance.
        Amendment No.: 201
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39455) The October 31, 1995, facsimile transmission was clarifying in 
    nature and did not affect the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated November 14, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: June 7, 1995
        Brief description of amendment: This amendment revises Technical 
    Specification 3/4.9.4, Refueling Operations - Containment Penetrations; 
    
    
    [[Page 62501]]
    Bases 3/4.9.4, Containment Penetrations; and Limiting Condition for 
    Operation (LCO) 3.9.4.b to allow both doors of the containment 
    personnel airlock to be open during core alterations or movement of 
    irradiated fuel within the containment, provided that certain specified 
    conditions are meet. Additional changes revise or clarify TS LCO 
    3.9.4.c, TS Action 3.9.4.a, and TS Surveillance Requirement 4.9.4, and 
    modify the associated Bases.
        Date of issuance: November 17, 1995
        Effective date: November 17, 1995
        Amendment No.: 202
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39454) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 17, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location:  University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: December 6, 1994
        Brief description of amendments: These changes revise Technical 
    Specifications to allow appropriate remedial action for high 
    particulate levels in the diesel generator fuel oil inventory and other 
    out-of-limit properties in new diesel generator fuel oil that has been 
    added to the existing diesel generator fuel oil storage inventory.
        Date of issuance: November 17, 1995
        Effective date: November 17, 1995
        Amendment Nos.: Unit 1 - Amendment No. 43; Unit 2 - Amendment No. 
    29
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6311) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 17, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Callaway 
    County, Missouri
    
        Date of amendment request: January 13, 1995
        Brief description of amendment: The amendment revises Technical 
    Specifications (TS) 3.3.1 and 3.3.2 to relocate Tables 3.3-2 and 3.3-5, 
    which provide the response time limits for the reactor trip system and 
    the engineered safety features actuation system instruments, from the 
    TS to the updated Final Safety Analysis Report (FSAR). The amendment 
    also relocates the Bases discussion for TS 3.3.1 and TS 3.3.2 to 
    Section 16.3 of the updated FSAR.
        Date of issuance: November 22, 1995
        Effective date: November 22, 1995, to be implemented within 30 days 
    of issuance.
        Amendment No.: 104
        Facility Operating License No. NPF-30. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8741) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 22, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room locations: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: June 6, 1995
        Brief description of amendment: The amendment modifies the Index of 
    the WNP-2 Technical Specifications by deleting reference to the Bases 
    pages.
        Date of issuance: November 24, 1995
        Effective date: November 24, 1995
        Amendment No.: 143
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37102) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 24, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: September 13, 1995, and October 
    19, 1995, as supplemented by letter dated October 25, 1995
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) Section 15.1, ``Definitions,'' TS Section 15.3.1.G, 
    ``Operational Limitations'' (and basis), and TS Figure 15.2.1-2, 
    ``Reactor Core Safety Limits, Point Beach Unit 2.'' The changes reduce 
    the reactor coolant system raw measured total flow rate limit and 
    reflect new reactor core safety limits for Unit 2.
        Date of issuance: November 17, 1995
        Effective date: November 17, 1995
        Amendment Nos.: 165 and 169
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Technical Specifications. Public comments requested as to 
    proposed no significant hazards consideration: Yes (60 FR 54527 dated 
    October 24, 1995). That notice provided an opportunity to submit 
    comments on the Commission's proposed no significant hazards 
    consideration determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by November 24, 
    1995, but indicated that if the Commission makes a final no significant 
    hazards consideration determination any such hearing would take place 
    after issuance of the amendment. The Commission's related evaluation of 
    the amendment, finding of exigent circumstances, and final 
    determination of no significant hazards consideration is contained in a 
    Safety Evaluation dated November 17, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: September 14, 1995
        Brief description of amendment: The amendment revised Technical 
    Specification 3/4.5.5 to increase the allowed outage time for 
    adjustment of boron concentration for the refueling water storage tank 
    from 1 hour to 8 hours.
        Date of issuance: November 13, 1995 
        
    [[Page 62502]]
    
        Effective date: November 13, 1995, to be implemented within 30 days 
    of issuance.
        Amendment No.: 91
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52936) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 13, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (exigent public announcement or emergency 
    circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By January 5, 1996, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above. 
    
    [[Page 62503]]
    
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: November 9, 1995, as 
    supplemented by letters dated November 13, 1995, and November 16, 1995
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) Section 15.4.2, ``In-Service Inspection of Safety 
    Class Components,'' to incorporate a new steam generator tube 
    acceptance criterion for the Unit 2 steam generators. This criterion 
    allows tubes that are degraded or defective in a location (within the 
    tubesheet) that does not affect the structural integrity of the tube to 
    remain in service. The applicable basis is also changed.
        Date of issuance: November 22, 1995
        Effective date: November 22, 1995
        Amendment Nos.: 166 and 170
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications. Public comments requested as to 
    proposed no significant hazards consideration: No The Commission's 
    related evaluation of the amendments, finding of emergency 
    circumstances, and final determination of no significant hazards 
    consideration are contained in a Safety Evaluation dated November 22, 
    1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Ernest L. Blake, Jr., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: Gail H. Marcus
        Dated at Rockville, Maryland, this 29th day of November 1995.
        For the Nuclear Regulatory Commission
    Elinor G. Adensam,
    Deputy Director, Division of Reactor Projects - III/IV, Office of 
    Nuclear Reactor Regulation
    [Doc. 95-29540 Filed 12-5-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Effective Date:
11/21/1995
Published:
12/06/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X95-31206
Dates:
November 21, 1995
Pages:
62485-62503 (19 pages)
PDF File:
x95-31206.pdf