94-29925. Biweekly Notice  

  • [Federal Register Volume 59, Number 234 (Wednesday, December 7, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 94-29925]
    
    
    [[Page Unknown]]
    
    [Federal Register: December 7, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
     
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from November 14, 1994, through November 25, 
    1994. The last biweekly notice was published on November 23, 1994 (59 
    FR 60377).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By January 6, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: October 25, 1994
        Description of amendments request: The proposed change would delete 
    the remainder of Appendix B, Environmental Technical Specifications, 
    including section 2/3.3.1, Water Level in the Discharge Canal, and 
    Section 2/3.4, Meteorology.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Hydraulic - Water level in the Discharge Canal
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The deletion of the discharge canal 
    specification of 4.5 [plus or minus] 1 ft mean sea level (msl) with 
    daily monitoring still leaves the operating restrictions delineated 
    in Updated Final Safety Analysis Report (UFSAR) Section 2.4.8.3.3 
    (4.5 [plus or minus] 2 ft msl) and the National Pollutant Discharge 
    Elimination System (NPDES) permit requirements to minimize the 
    impact of the discharge canal on the local groundwater supply. As 
    stated in this UFSAR section, the effect on the local ground water 
    regime will be minimal within this band. Level recorders in the 
    control room facilitate the continued monitoring the discharge canal 
    level in excess of the Appendix B Environment Technical 
    Specification (ETS) listed daily surveillance. This change in no way 
    affects the design or operation of equipment that could initiate or 
    mitigate any accident previously evaluated.
        2. The proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The discharge canal level is an environmental concern 
    with the effects of a spill of radioactive liquids (UFSAR Section 
    2.4.12.3) being a path to the intake canal, due to the areas natural 
    gradient. With the estimated travel time for the liquid to reach the 
    canal (intake) at 60 years, and the large flow rate the degree of 
    dilution is such that this does not pose a threat to local wells. 
    The amendment would not affect the operation or design of any plant 
    equipment; therefore, no new credible accidents are created. In 
    addition, the proposed amendment would not affect the capability of 
    the response systems to mitigate the consequences of any accident 
    previously evaluated; therefore, no new or different accident would 
    result from this change.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety. The existence of these ETS does not 
    provide a margin of safety related to the nuclear operation of the 
    site. No safety limits are affected by this change. Therefore, this 
    amendment would not result in a reduction in any margin of safety.
        Meteorology
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The deletion of the meteorology specification 
    still leaves the program delineated in UFSAR Section 2.3.3, Onsite 
    Meteorological Measurements Program, and reporting/recording of the 
    hourly meteorological data required to support Technical 
    Specification 6.9.1.10.a, Semiannual Radioactive Effluent Release 
    Report. This program is based on the meteorological monitoring 
    program described in Regulatory Guide 1.23, and NUREG-0654. While 
    the existing ETS 30 day reporting requirement for extended out-of-
    service time and shiftly manual acquisition of data during batch or 
    accidental releases are not otherwise covered, the program does 
    contain the Regulatory Guide 1.23 reference to 90% data recovery and 
    a backup phone line is available for data retrieval. This proposed 
    amendment in no way affects the design or operation of equipment 
    that could initiate or mitigate any accident previously evaluated.
        2. The proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The meteorological monitoring program is specified in 
    UFSAR Section 2.3.3. The amendment would not affect the operation or 
    design of any plant equipment; therefore, no new credible accidents 
    are created. In addition, the proposed amendment would not affect 
    the capability of the response systems to mitigate the consequences 
    of any accident previously evaluated nor would the amendment reduce 
    the effectiveness of the Emergency Response Plan; therefore, no new 
    or different accident would result from this change.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety. The meteorological ETS does not 
    provide any additional margin of safety related to the operation of 
    a nuclear plant. The meteorological program established in the UFSAR 
    covers the requirements stated in Appendix E to 10 CFR 50 by 
    providing meteorological systems adequate for determining the 
    magnitude of, and for continuously assessing the impact of, the 
    release of radioactive materials to the environment. The 
    meteorological instrumentation is used to measure environmental 
    parameters which may affect distribution of fission products and 
    gases following a Design Basis Accident (DBA); however, it is not a 
    primary success path for the mitigation of a DBA. No safety limits 
    are affected by this change. Therefore, this amendment would not 
    result in a reduction in any margin of safety.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: William H. Bateman
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: October 28, 1994
        Description of amendments request: The proposed changes would 
    revise the Technical Specifications to increase the surveillance test 
    intervals and allowable out-of-service times for selected 
    instrumentation addressed in Section 3/4.3. The proposed changes would 
    permit specified channel functional tests to be conducted quarterly 
    rather than weekly or monthly. Specifically, the proposed changes would 
    revise the surveillance test intervals and allowable out-of-service 
    times for the reactor protection system instrumentation, isolation 
    actuation instrumentation, emergency core cooling system actuation 
    instrumentation, control rod withdrawal block instumentation, control 
    room emergency ventilation system instrumentation, anticipated 
    transient without scram - recirculation pump trip system 
    instrumentation, end-of-cycle recirculation pump trip system 
    instrumentation, and reactor core isolation cooling system actuation 
    instrumentation, in accordance with NRC-approved General Electric 
    Company Licensing Topical Reports and NUREG-1433, Standard Technical 
    Specifications, General Electric Plants, BWR/4.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) Operation of Brunswick Steam Electric Plant, Units 1 and 2, 
    in accordance with the proposed amendment, would not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The generic Licensing Topical Report, NEDC-30851P-A, assessed 
    the impact of changing RPS surveillance test intervals (STIs) and 
    allowable out-of-service times (AOTs) on the RPS failure frequency, 
    the scram frequency and equipment cycling. Specifically, Section 
    5.7.4, ``Significant Hazards Assessment'' of NEDC-30851P-1 states:
        ``Fewer challenges to the safeguards system, due to less 
    frequent testing of the RPS, conservatively results in a decrease of 
    approximately one percent in core damage frequency''. This decrease 
    is based upon the following:
        * Based on the plant-specific experience presented in Appendix 
    J, the estimated reduction in scram frequency (0.3 scrams/yr) 
    represents a 1 to 2 percent decrease in core damage frequency based 
    on the BWR plant specific Probabilistic Risk Assessments (PRAs) 
    listed in Table 5-8.
        * The increase in core damage frequency due to less frequent 
    testing is less than one percent. This increase is even lower (less 
    than 0.01 percent) when the changes resulting from the 
    implementation of the Anticipated Transients Without Scram (ATWS) 
    rule are considered. Therefore, this increase is more than offset by 
    the decrease in CDF due to fewer scrams.
        * The effect of reducing unnecessary cycles on RPS equipment, 
    although not easily quantifiable also results in a decrease in core 
    damage frequency.
        * The overall impact on core damage frequency of the changes in 
    allowable out-of-service time is negligible.''
        From this generic analysis, the BWR Owners' Group concluded and 
    CP&L concurs that the proposed changes do not significantly increase 
    the probability or consequences of an accident previously evaluated, 
    since the increase in probability of a a scram failure due to RPS 
    unavailablity is insignificant. The overall probability of an 
    accident is decreased as the time the RPS instrumentation logic 
    operates undisturbed is increased, resulting in fewer inadvertent 
    scrams during testing and repair. The proprietary plant-specific 
    analysis contained in this submittal (Enclosure 6) demonstrates 
    that, although BSEP Units 1 and 2 differ from the generic plant 
    analyzed in LTR NEDC-30851P-A, the net effect of the plant-specific 
    differences does not alter the generic conclusions.
        The generic Licensing Topical Reports, NEDC-30851P-A, Supplement 
    2 and NEDC 31677P-A, assessed the impact of changing STIs and AOTs 
    for BWR Isolation Instrumentation. Section 4.0, ``Summary of 
    Results,'' of NEDC-30851P-A, Supplement 2 states:
        ``The results indicate that the effects on probability of 
    failure to initiate isolation are very small and the effects on 
    probability or frequency of failure to isolate are negligible in 
    nearly every case. In addition, the results indicate that increasing 
    the AOT to 24 hours for tests and repairs has a negligible effect on 
    the probability of failure of the isolation function. These combined 
    with changes to the testing intervals and allowable out-of service 
    times for RPS and ECCS instrumentation provide a net improvement to 
    plant safety and operations.''
        and Section 5.6, ``Assessment of Net Effect of Changes,'' of 
    NEDC-31677P-A states:
        ``A reduction in core damage frequency (CDF) of at least as much 
    as estimated in the ECCS instrumentation analysis can be expected 
    when the isolation actuation instrumentation STIs are changed from 
    one month to three months. The chief contributor to this reduction 
    is the channel functional tests for the MSIVs. Inadvertent closure 
    of the MSIVs will cause an unnecessary plant scram. This reduction 
    in CDF more than compensates for any small incremental increase (10% 
    or 1.0E-07/year) in calculated isolation function failure frequency 
    when the STI is extended to three months.''
        From this generic analysis, the BWR Owners' Group concluded and 
    CP&L concurs that the proposed changes do not significantly increase 
    the consequences of an accident previously evaluated, since the 
    increase in probability of an isolation failure due to isolation 
    instrumentation unavailability is insignificant. For those 
    parameters common to RPS, the overall probability of an accident is 
    actually decreased as the time the RPS instrumentation logic 
    operates undisturbed is increased, resulting in less inadvertent 
    scrams during testing and repair. The plant-specific evaluation 
    provided with this submittal (Enclosure 8) demonstrates that the 
    conclusions of the generic analyses are applicable to BSEP Units 1 
    and 2.
        The generic Licensing Topical Report, NEDC-30936P-A (Parts 1 and 
    2), assessed the impact of changing STIs and AOTs for all BWR ECCS 
    Actuation Instrumentation. Section 4.0, ``Technical Assessment of 
    Changes,'' of NEDC-30936P-A (Part 2) states:
        ``The results indicate an insignificant (less than 5E-7 per 
    year) increase in water injection function failure frequency when 
    STIs are increased from 31 days to 92 days, AOTs for repair of the 
    ECCS actuation instrumentation are increased from one hour to 24 
    hours, and AOTs for surveillance testing are increased from two to 
    six hours. For all four BWR models the increase represents less than 
    4% increase in failure frequency. However, when other factors which 
    influence the overall plant safety are considered, the net result is 
    judged to be an improvement in plant safety.''
        From this generic analysis, the BWR Owners' Group concluded and 
    CP&L concurs that the proposed changes do not significantly increase 
    the probability or consequences of an accident previously evaluated, 
    since the increase in probability of a water injection failure due 
    to ECCS instrumentation unavailability is insignificant and the net 
    result is judged to be an improvement in plant safety. The plant-
    specific analysis contained in this submittal (Enclosure 7) 
    demonstrates that, although BSEP Units 1 and 2 differ from the 
    generic model analyzed in LTR NEDC-30936P-A, the net effect of the 
    plant-specific differences does not alter the generic conclusions. 
    The generic Licensing Topical Reports, NEDC-30851P-A, Supplement 1, 
    and GENE-770-06-1-A assessed the impact of changing Control Rod 
    Block STIs and AOTs on Rod Block failure frequency. GENE-770-06-1-A 
    also assessed the impact of changing STIs and AOTs on ATWS-RPT and 
    EOC-RPT failure frequency. Section 5 (Brookhaven National 
    Laboratory's Technical Evaluation Report - Attachment 2 to the NRC 
    SER) of NEDC-30851P-A, Supplement 1 states:
        1``The BWR Owners' Group proposed changes to the Technical 
    Specifications concerning the test requirements for BWR control rod 
    block instrumentation. The changes consist of increasing the 
    surveillance test intervals from one to three months. These test 
    interval extensions are consistent with the already approved changes 
    to STIs for the Reactor Protection System. The technical analysis 
    reviewed and verified as documented herein indicates that there will 
    be no significant changes in the availability of the control rod 
    block function if these changes are implemented. In addition, there 
    will be a negligible impact on the plant core melt frequency due to 
    the decreased testing.''
        and Section 2.0, ``Summary'' of GENE-770-06-1-A states:
        ``Technical bases are provided for selected proposed changes to 
    the instrumentation STIs and AOTs that were identified in the BWROG 
    Improved BWR Technical Specification activity. These STI and AOT 
    changes are consistent with approved changes to the RPS, ECCS, and 
    isolation actuation instrumentation. These proposed changes do not 
    result in a degradation to overall plant safety.''
        Based on the generic analysis in NEDC-30851P-A, Supplement 1, 
    the BWR Owners' Group concluded and CP&L concurs that the proposed 
    changes to Control Rod Withdrawal Block instrumentation do not 
    significantly increase the probability or consequences of an 
    accident previously evaluated. Also, based on the generic assessment 
    in GENE-770-06-1-A, the BWR Owners' Group concluded and CP&L concurs 
    that the proposed changes to the ATWS-RPT and EOC-RPT 
    instrumentation do not significantly increase the probability or 
    consequences of an accident previously evaluated.
        Bases contained in GE Topical Report GENE-770-06-2P-A, assessed 
    the impact of changing STIs and AOTs on BWR RCIC failure frequency. 
    Section 2.0, ``Summary'' of GENE-770-06-2P-A states:
        ``The STI and AOT changes to the RCIC actuation instrumentation 
    are justified based on their small effect on the water injection 
    function unavailability and consistency with comparable changes to 
    actuation instrumentation for the other ECCS subsystems.''
        On this basis, the BWR Owners' Group concluded and CP&L concurs 
    that the proposed changes to RCIC instrumentation do not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        2) Operation of Brunswick Steam Electric Plant, Units 1 and 2, 
    in accordance with the proposed amendment, would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed changes do not alter the physical characteristics 
    or function of any plant systems or components and they do not 
    introduce any new mode of operation. Therefore, system and component 
    performance would not be challenged in a manner that could create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3) Operation of Brunswick Steam Electric Plant, Units 1 and 2, 
    in accordance with the proposed amendment, would not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed and approved the generic studies 
    contained in the LTRs and has concurred with the BWR Owners' Group 
    that the proposed changes do not significantly affect the 
    probability of failure or availability of the affected Instrument 
    Systems. The proposed changes to AOTs provide realistic times to 
    complete the required actions without increasing the overall 
    instrument failure frequency. Likewise, the extended STIs do not 
    result in significant changes in the probability of instrument 
    failure. Furthermore, the proposed changes will reduce the 
    probability of test-induced plant transients and equipment failures. 
    Finally, instrument setpoint drift will remain within present 
    tolerances, thereby assuring that the margin of safety, as 
    demonstrated by applicable safety analyses, remains unchanged. 
    Therefore, it is concluded that the proposed changes would not 
    result in a reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: William H. Bateman
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: November 4, 1994
        Description of amendment request: The requested amendment will 
    change the testing frequency of the turbine overspeed protection valves 
    from monthly to quarterly.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The requested change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The requested change will have no influence on the 
    probability or consequences of an accident previously evaluated. The 
    accident of concern to this requested change is a turbine overspeed 
    with missile generation impacting safety related components or 
    structures. The evaluation in WCAP-11525 shows that the probability 
    of a missile ejection incident will not be affected with the 
    requested frequency reduction to the turbine overspeed protection 
    valve surveillance test. There is no change to the consequences of 
    the event as the postulated accident event is unchanged. 
    Accordingly, the requested change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The requested change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The change affects the test interval for the turbine 
    overspeed protection valves and does not change the design, 
    operation, or failure modes of the valves and other components in 
    the turbine overspeed protection system. Therefore, the requested 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The requested change does not involve a significant reduction 
    in the margin of safety. The probability of turbine overspeed with 
    an extension of the testing interval has been determined to be 
    within applicable acceptance criteria. The change does not affect 
    the design, operation, or failure modes of the valves or other 
    components in the turbine overspeed protection system. Accordingly, 
    the requested change will not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: William H. Bateman
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: November 7, 1994
        Description of amendment request: The proposed amendment would 
    allow an increase to the allowable nominal fuel enrichment from 4.2 to 
    5.0 weight percent Uranium-235 (w/o U-235). The changes include: (1) 
    increasing the allowable storage enrichment in Region 1 and allowing 
    the use of Integral Fuel Burnable Absorbers (IFBAs) for reactivity 
    equivalencing, (2) revising the Region 2 discharge burnup curve to 
    include nominal fuel enrichments up to 5.0 w/o U-235, and (3) making 
    editorial changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes to Section 5 of Technical Specifications do 
    not affect any accident initiators or precursors and do not change 
    or alter the design assumptions for the systems or components used 
    to mitigate the consequences of an accident. The fuel enrichment 
    increase will not affect reactor operation or the core design 
    methods. The physical characteristics of the fuel assemblies are not 
    changed, and fuel assembly movement will continue to be controlled 
    by approved fuel handling procedures. Reload core designs will 
    continue to be performed on a cycle by cycle bases as part of the 
    reload safety evaluation process, using NRC approved codes and 
    methods. Each reload design is evaluated to confirm that the cycle 
    core design adheres to the limits that exist in the accident 
    analyses and Technical Specifications to ensure that reactor 
    operation is acceptable.
        The proposed changes are consistent with the analysis performed 
    in the ``Criticality Analysis of Byron and Braidwood Station Fuel 
    Storage Racks.'' The analysis was revised in June 1994 to include 
    boraflex gaps and shrinkage. The revised analysis is provided in the 
    proposed Technical Specification amendment. The analysis methodology 
    has been previously accepted by the NRC and is consistent with the 
    appropriate standards to establish the Keff limit for storage 
    racks and to calculate the maximum Keff. The reanalysis 
    addresses the most limiting postulated accident of a misloaded fuel 
    assembly and has shown that having at least 300 ppm of soluble boron 
    offsets any positive reactivity impacts for any of the postulated 
    accidents. The concentration of boron in the spent fuel pool water, 
    which is administratively controlled, is sufficient to maintain 
    Keff less than or equal to 0.95. The analysis is bounding for a 
    dropped fuel assembly on top of a rack or between rack modules, loss 
    of cooling systems, and reduction the fuel pool temperature to less 
    than 50 deg.F. The proposed changes do not impact any other accident 
    previously evaluated in the [Updated Final Safety Analysis Report] 
    UFSAR. There is no postulated accident that could cause reactivity 
    to increase beyond the analyzed conditions in the spent fuel racks.
        There is no impact on the ability of the Spent Fuel Pool cooling 
    system to maintain the bulk pool temperature within limits. The 
    UFSAR analysis performed to calculate the maximum fuel cladding 
    temperature and spent fuel pool cooling include assumptions which 
    bound the use of more highly enriched fuel assemblies. Although fuel 
    enrichment is not a specific assumption in any of these analyses, 
    the heat load of a typical core offload may change with higher 
    enrichments. The average burnup of the offload will be increased 
    since few assemblies will be used per cycle; however, the new heat 
    load will continue to be [bound] by the UFSAR analysis because the 
    spent fuel pool racks have been analyzed for a total core offload 
    with all fuel assemblies having 4.5 years of operating time.
        The radiological consequences analysis continues to bound the 
    licensed fuel burnup and enrichment at Byron and Braidwood stations. 
    The radiological consequences analysis results are a function of the 
    core inventory of radioactive isotopes. Since the maximum fuel 
    burnup limits and fuel peaking factors will not be exceeded, the 
    assumed fission product inventory will remain valid; therefore, the 
    limits of 10 CFR [Part] 100 continue to be met. Additionally, Byron 
    and Braidwood addressed the issue of the impact on the radiation 
    levels at the pool surface to the worker during non-accident 
    conditions. These conditions are not changed as [a] result of this 
    submittal, because the average fuel assembly burnup limit (isotopic 
    inventory) and maximum power produced in each fuel assembly will not 
    be changed by the increased fuel enrichment.
        B. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not affect the design or operation of 
    any system, structure, or component in the plant. There are no 
    changes to parameters governing plant operation; no new or different 
    type of equipment will be installed. Each reactor core design will 
    continue to meet all design requirements; operation of the core will 
    not be affected. No modifications to the spent fuel pool are being 
    pursued and the fuel parameters used in the analysis remain 
    bounding. The method and manner in which the fuel will be stored in 
    the spent fuel pool has not changed. The proposed changes ensure 
    that 17X17 (Optimized Fuel Assembly, VANTAGE 5, VANTAGE +, and 
    PERFORMANCE +) fuel assemblies can be safely stored, maintaining a 
    Keff less than or equal to 0.95 under full water density 
    conditions, in both Regions 1 and 2 of the spent fuel pool. All 
    design criteria and criticality acceptance criteria continue to be 
    met. The reanalysis addresses the most limiting postulated accident 
    (misloaded fuel assembly) and has shown that having at least 300 ppm 
    of soluble boron offsets any positive reactivity impacts for any of 
    the postulated accidents. The level of boron in the spent fuel pool 
    water, which is administratively controlled, is sufficient to 
    maintain Keff less than or equal to 0.95. The reanalysis to 
    increase the storage enrichment of fuel in Regions 1 and 2 of the 
    spent fuel pool does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Additionally, approval of this amendment will not create a new 
    accident with regards to the new fuel storage vault which is 
    designed to handle the increased enrichment. The Byron and Braidwood 
    new fuel vaults were previously analyzed using NRC accepted 
    criticality analysis methodology in June 1989. This analysis was 
    performed to increase the storage enrichment of the New Fuel Vault 
    to 5.0 w/o U-235. The New Fuel Vault analysis was submitted to the 
    NRC and is the current licensing basis.
        C. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect the margin of safety for any 
    Technical Specification. All reactor design criteria will continue 
    to be met. The methodologies used in the accident analyses have been 
    accepted previously by the NRC and all criticality acceptance 
    criteria have been met under all assumed conditions (normal and 
    accident). The design basis for preventing criticality outside the 
    reactor is that, including uncertainties, there is a 95 percent 
    probability at a 95 percent confidence level that the effective 
    neutron multiplication factor, Keff, of the fuel assembly array 
    will be less than 0.95 as recommended by ANSI 57.2-1983 and OT 
    Position Paper for Review and Acceptance of Spent Fuel Storage and 
    Handling Applications, dated April 14, 1978. The analyses for both 
    Regions 1 and 2 fuel storage were verified to meet the above design 
    basis.
        The criticality analysis for Regions 1 and 2 has been revised to 
    allow for storage of fuel assemblies with enrichments up to 5.0 w/o 
    U-235. The proposed Technical Specification changes include those 
    changes necessary to maintain Keff less than or equal to 0.95, 
    including conservative allowances for uncertainties and biases, when 
    the pool is flooded with unborated water. The proposed changes 
    include a requirement for fuel assemblies with enrichments above 4.2 
    w/o U-235 to contain sufficient integral fuel burnable absorbers 
    such that the maximum reference fuel K infinity is less than or 
    equal to 1.470 in unborated water at 68 deg.F due to restrictions on 
    spent fuel storage. Should a postulated accident occur which causes 
    a reactivity increase in the Byron and Braidwood Spent Fuel Pools, 
    Keff will be maintained less than or equal to 0.95 due to the 
    presence of at least 300 ppm of soluble boron in the spent fuel 
    pool. The proposed changes do not affect any plant safety parameters 
    or setpoints.
        The proposed changes ensure that the design basis for preventing 
    criticality in the fuel storage areas is preserved, and fuel cycle 
    designs will continue to be analyzed using NRC accepted codes and 
    methods to ensure the design bases are satisfied.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: Robert A. Capra
    
    Connecticut Yankee Atomic Power Company (CYAPCO), and Northeast 
    Nuclear Energy Company (NNECO), Docket Nos. 50-213 and 50-245, 
    Haddam Neck Plant, and Millstone Nuclear Power Station, Unit 1, 
    Middlesex County, and New London County, Connecticut
    
        Date of amendment request: October 31, 1994
        Description of amendment request: The proposed amendments would 
    renew the existing license conditions for both plants to implement and 
    maintain Integrated Implementation Schedule (IIS) Program Plans (the 
    Program Plan). The Program Plans provide a methodology to be followed 
    for scheduling plant modifications and engineering evaluations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        YAPCO and NNECO have reviewed the proposed changes in accordance 
    with 10 CFR 50.92 and conclude that the changes do not involve a SHC 
    [significant hazards consideration]. The basis for this conclusion 
    is that the three criteria of 10 CFR 50.92(c) are not compromised. 
    The proposed changes do not involve an SHC because the changes would 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        Operation of the facilities in accordance with these proposed 
    changes would require the implementation of the IIS methodology 
    described in the Program Plans. As such, it requires that CYAPCO and 
    NNECO establish an administrative means for tracking, prioritizing, 
    and scheduling NRC-required plant modifications and engineering 
    evaluations, and licensee identified plant improvement projects. 
    This methodology is intended to enhance plant safety by more 
    effectively controlling the number and scheduling of plant 
    modifications, thereby assuring that issues required for safe 
    operation of the plants receive priority and are completed in a 
    timely manner. Because the license conditions address only an 
    administrative scheduling mechanism, it does not affect directly the 
    design or operation of the plant. Therefore, no accident analyses 
    are affected and the proposed changes do not increase the 
    probability or consequences of any previously evaluated accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed license conditions establish a requirement related 
    to scheduling of modifications and engineering evaluations. Because 
    the license conditions address only an administrative scheduling 
    mechanism, they do not affect directly the design or operation of 
    the plants. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from those 
    previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The proposed license conditions renew administrative 
    requirements intended to enhance public safety and reliable plant 
    operation. The proposed license conditions do not affect any 
    accident analyses, directly modify the plant configurations, or 
    change the way the plants are operated. The methodologies are 
    intended to enhance plant safety by more effectively controlling the 
    number and scheduling of plant modifications, thereby assuring that 
    issues required for safe operation of the plants receive priority 
    and are completed in a timely manner. Because the license conditions 
    address only an administrative scheduling mechanism, they do not 
    affect directly the design or operation of the plants. Therefore, 
    the proposed changes do not involve a reduction in any margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, Connecticut 06457, for the Haddam Neck Plant, and 
    the Learning Resource Center, Three Rivers Community-Technical College, 
    Thames Valley Campus, 574 New London Turnpike, Norwich, CT 06360, for 
    Millstone Unit 1.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: August 5, 1994, as supplemented on 
    November 17, 1994.
        Description of amendment request: This amendment is an additional 
    followup to the amendment request of May 29, 1992, published in the 
    Federal Register on July 8, 1992 (57 FR 30242), which changed the 
    Technical Specifications (TSs) Section 1.0, Definitions, to accommodate 
    a 24-month fuel cycle and which proposed the extension of the test 
    intervals for specific surveillance tests. This amendment proposes 
    extending the surveillance intervals to 24 months for the following 
    additional surveillance tests:
        (1) Charging Flow Instrumentation
        (2) Containment Sump, Recirculation Sump, and Reactor Cavity 
    Continuous Level Instrument Channels
        (3) Auxiliary Feedwater Flow Rate Channel
        (4) Control Room Air Filtration System
        (5) Post Accident Containment Venting System
        (6) Liquid Rad-Waste Flow Channel
        (7) Steam Generator Blowdown Flow Channel
        (8) Liquid Waste Distillate Tank Level Channels
        (9) Primary Water Storage Tank Level Instrumentation
        (10) Flow Rate Monitors; Plant Vent (Unit 2) and Stack Vent (Unit 
    1)
        (11) Stack Vent Noble Gas Activity Monitor (R-60)
        (12) High Pressure Water Fire Protection System
        (13) Fire Protection System Diesel Engine
        (14) Electrical Tunnel, Diesel Generator Building, and Containment 
    Fan Cooler Fire Protection Spray Systems; (A) System Functional Test 
    and (B) Spray Header Visual Inspection
        (15) Penetration Fire Barriers
        (16) Smoke Detectors/Electrical Penetration Area Inside Containment
        (17) Functional Testing of Containment Sump Pumps
        The changes requested by the licensee are in accordance with 
    Generic Letter 91-04, ``Changes in Technical Specification Surveillance 
    Intervals to Accommodate a 24-Month Fuel Cycle.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Charging Flow Instrumentation
        The proposed change does not involve a significant hazards 
    consideration since:
        1. A significant increase in the probability or consequences of 
    an accident previously evaluated will not occur.
        It is proposed that the channel calibration frequency for the 
    Charging Flow instrumentation be changed from 18 months (+25%) to 
    every 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    channel statistical error resulting from a 30 month operating cycle. 
    The existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any accident previously evaluated has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a channel 
    statistical allowance which exceeds the current margin. Plant 
    equipment will provide protective functions to assure that Safety 
    Analysis limits are not exceeded. This will prevent the possibility 
    of a new or different kind of accident from any previously evaluated 
    from occurring.
        3. A significant reduction in a margin of safety is not 
    involved.
        The above change in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds current margin. This margin, which is 
    equivalent to the existing margin, is necessary to assure that 
    protective safety functions will occur so that Safety Analysis 
    limits are not exceeded.(2) Containment Sump, Recirculation Sump, 
    and Reactor Cavity Continuous Level Instrument Channels
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the calibration and test frequency for the 
    Containment Sump, Recirculation Sump and Reactor Cavity continuous 
    level monitoring instrument channels be revised from every 18 months 
    (+25%) to 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    channel statistical error resulting from a 30 month operating cycle. 
    The existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a channel 
    statistical allowance which exceeds current margin. Plant equipment 
    will provide protective functions to assure that Safety Analysis 
    limits are not exceeded. This will prevent the possibility of a new 
    or different kind of accident from any previously evaluated from 
    occurring.
        3. There has been no reduction in the margin of safety.
        The above change in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds current margin. This margin is necessary to 
    assure that protective safety functions will occur so that safety 
    analysis limits are not exceeded.
        (3) Auxiliary Feedwater Flow Rate Channel
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the calibration frequency for the Auxiliary 
    Feedwater Flow Rate channel be revised from 18 months (+25%) to 24 
    months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists between the existing 
    technical specification limits and the licensing basis Safety 
    Analysis limit to accommodate the channel statistical error 
    resulting from a 30 month operating cycle. The existing margin 
    between the Technical Specification limit and the Safety Analysis 
    limit provides assurance that plant protective actions will occur as 
    required. It is therefore concluded that changing the surveillance 
    interval from 18 months (+25%) to 24 months (+25%) will not result 
    in a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a channel 
    statistical allowance which exceeds the current margin between the 
    existing Technical Specification limit and the Safety Analysis 
    limit. Plant equipment, which will be set at (or more conservatively 
    than) Technical Specification limits, will provide protective 
    functions to assure that safety analysis limits are not exceeded. 
    This will prevent the possibility of a new or different kind of 
    accident from any previously evaluated from occurring.
        3. There has been no reduction in the margin of safety.
        The above change in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds the margin which exists between the current 
    Technical Specification limit and the licensing basis Safety 
    Analysis limit. This margin, which is equivalent to the existing 
    margin, is necessary to assure that protective safety functions will 
    occur so that Safety Analysis limits are not exceeded.
        (4) Control Room Air Filtration System
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the surveillance frequency for the Control 
    Room Air Filtration System be changed from every 18 months (+25%) to 
    every 24 months (+25%).
        For the flow tests, data from 1986 to date indicates that the 
    Control Room Filtration System performed in an acceptable manner 
    when surveilled on an 18 month (+25%) basis. The only discrepancy 
    was due to a hardware error and was independent of the time between 
    surveillances. Per Generic Letter 91-04, this past test history 
    provides an adequate basis to conclude that an extended operating 
    cycle would have minimal impact upon the flow characteristics of the 
    Control Room Filtration System. The modification of the filtration 
    system in 1993 only enhanced system performance.
        With regard to the absorbance properties of the charcoal, 
    previous test data highlights a problem occurring during the 1986-
    1987 period which subsequent testing confirms was adequately 
    resolved.
        With the 1993 modification which increased the carbon bed 
    thickness from 1'' to 4'', performance can only be enhanced.
        Therefore, it is concluded that a significant increase in the 
    probability or consequences of an accident previously evaluated will 
    not be incurred by changing the surveillance interval from 18 months 
    (+25%) to 24 months (+25%).
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        A review of past historical surveillance data over 7 years 
    indicates no failures which were time dependent. The modification, 
    which was performed in 1993, can only enhance performance of the 
    system. New fans, an increased charcoal bed thickness, and new HEPA 
    [high-efficiency particulate air] filters will increase the 
    reliability of the system. Thus, it is concluded that the 
    possibility of a new or different kind of accident than that 
    previously evaluated has not been created.
        3. There has been no significant reduction in the margin of 
    safety.
        Past test data validated the acceptability of the previous air 
    filtration system for an extended surveillance interval. The 
    modification performed in 1993 will only enhance the reliability and 
    performance of the air filtration system. Thus, it is concluded that 
    a significant reduction in the margin of safety is not involved.
        (5) Post Accident Containment Venting System
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the surveillance frequency for the Post 
    Accident Containment Venting system be revised from every 18 months 
    (+25%) to 24 months (+25%).
        A review of past test history from 1986 to date indicates that 
    the Post Accident Containment Venting System performed in a 
    satisfactory manner when the surveillance period was 18 months 
    (+25%). There was one discrepant condition noted in the 1989 test, 
    which, based upon subsequent tests in 1991 and 1993, does not appear 
    to have been age related. The 1989 observation concerning a gasket 
    is considered to be a one time only event and unlikely to reoccur as 
    a result of extending the surveillance interval from 18 months 
    (+25%) to 24 (+25%).
        An added consideration, in terms of safety significance, is the 
    fact that the Post Accident Containment Venting system is diverse 
    and redundant to the post accident hydrogen recombiners which are 
    themselves redundant and the primary means of reducing the post 
    accident hydrogen concentration within containment. The venting 
    system is not relied upon for containment pressure control.
        Due to the satisfactory past test history of the venting system, 
    together with its secondary role as a means of controlling post 
    accident hydrogen concentration, it is concluded that a significant 
    increase in the probability or consequences of an accident 
    previously evaluated will not be incurred by changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%).
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        A review of past historical surveillance data over 7 years 
    indicates no failures which are considered to be time dependent. 
    Although one discrepant condition was observed in the 1989 test it 
    was not repeated in subsequent surveillances. Per Generic Letter 91-
    04, this constitutes a sufficient basis for revising the 
    surveillance interval from 18 months (+25) to 24 months (+25%). This 
    extension in the operating interval is not expected to have an 
    impact upon the availability of the system. Thus, it is concluded 
    that the possibility of a new or different kind of accident 
    previously evaluated has not been created.
        3. There has been no reduction in the margin of safety.
        As past test data validates the presumption that an extended 
    operating cycle will not impact the availability of the Post 
    Accident Containment Venting Systems, it is concluded that a 
    significant reduction in the margin of safety is not involved.
        (6) Liquid Rad-Waste Flow Channel
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the channel calibration frequency for the 
    Liquid Rad-Waste Flow Channel be revised from every 18 months 
    (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    channel statistical error resulting from a 30 month operating cycle. 
    The existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a channel 
    statistical allowance which exceeds current margin. Plant equipment 
    will be set to provide protective functions to assure that Safety 
    Analysis limits are not exceeded. This will prevent the possibility 
    of a new or different kind of accident from any previously evaluated 
    from occurring.
        3. There has been no reduction in the margin of safety.
        The above change in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds the allowable operating margin. This margin, 
    which is equivalent to the existing margin, is necessary to assure 
    that protective safety functions will occur so that Safety Analysis 
    limits are not exceeded.
        (7) Steam Generator Blowdown Flow Channel
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the channel calibration frequency for the 
    Steam Generator Blowdown Flow channel be revised from every 18 
    months (+25%) to every 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    channel statistical error resulting from a 30 month operating cycle. 
    The existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a channel 
    statistical allowance which exceeds the current margin. Plant 
    equipment will provide protective functions to assure that Safety 
    Analysis limits are not exceeded. This will prevent the possibility 
    of a new or different kind of accident from any previously evaluated 
    from occurring.
        3. There has been no reduction in the margin of safety.
        The above change in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds the allowable operating margin. This margin, 
    which is equivalent to the existing margin, is necessary to assure 
    that protective safety functions will occur so that Safety Analysis 
    limits are not exceeded.
        (8) Liquid Waste Distillate Tank Level Channels
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the channel calibration frequency for the 
    Liquid Waste Distillate Tank level of tanks 13 and 14 be revised 
    from every 18 months (+25%) to every 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    channel statistical error resulting from a 30 month operating cycle. 
    The existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a channel 
    statistical allowance which exceeds current margin. Plant equipment 
    will be set to provided protective functions to assure that Safety 
    Analysis limits are not exceeded. This will prevent the possibility 
    of a new or different kind of accident from any previously evaluated 
    from occurring.
        3. There has been no reduction in the margin of safety.
        The above change in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds the allowable operating margin. This margin, 
    which is equivalent to the existing margin, is necessary to assure 
    that protective safety functions will occur so that safety analysis 
    limits are not exceeded.
        (9) Primary Water Storage Tank Level Instrumentation
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the channel calibration frequency for the 
    Primary Water Storage Tank Level instrumentation be changed from 
    every 18 months (+25%) to 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    surveillance has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    channel statistical error resulting form a 30 month surveillance. 
    The existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in surveillance interval will result in a 
    channel statistical allowance which can be accommodated over a 30 
    month operating cycle. Plant equipment, which will be set at (or 
    more conservatively than) Technical Specification limits, will 
    provide protective functions to assure that Safety Analysis limits 
    are not exceeded. This will prevent the possibility of a new or 
    different kind of accident from any previously evaluated from 
    occurring.
        3. There has been no significant reduction in the margin of 
    safety.
        The above changes in surveillance interval resulting from an 
    increased operating cycle will not result in a channel statistical 
    allowance which exceeds current margin. This margin is necessary to 
    assure that protective safety functions will occur so that Safety 
    Analysis limits are not exceeded.
        (10) Flow Rate Monitors; Plant Vent (Unit 2) and Stack Vent 
    (Unit 1)
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the calibration frequency for the flow rate 
    monitors for the Plant Vent (Unit 2) and the Stack Vent (Unit 1) be 
    revised from every 18 months (+25%) to every 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists to accommodate the 
    statistical error resulting from a 30 month operating cycle. The 
    existing margin provides assurance that plant protective actions 
    will occur as required. It is therefore concluded that changing the 
    surveillance interval from 18 months (+25%) to 24 months (+25%) will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in operating cycle length due to an 
    increased surveillance interval will not result in a statistical 
    allowance which exceeds the current margin. Plant equipment will be 
    calibrated to provide data to assure that safety analysis limits are 
    not exceeded. This will prevent the possibility of a new or 
    different kind of accident from an previously evaluated from 
    occurring.
        3. There has been no reduction in the margin of safety.
        The proposed change in the surveillance interval resulting from 
    an increased operating cycle will not result in a channel 
    statistical allowance which exceeds the allowable operating margin. 
    This margin, which is equivalent to the existing margin, is 
    necessary to assure that protective safety functions will occur so 
    that safety analysis limits are not exceeded.
        (11) Stack Vent Noble Gas Activity Monitor (R-60)
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the calibration frequency for the stack vent 
    noble gas activity monitor be revised from every 18 months (+25%) to 
    every 24 months (+25%).
        The current monitor replaced the previous monitor and therefore 
    there is only one refueling cycle surveillance data available which 
    proved to be satisfactory. The vendor recommends a calibration 
    period based on user experience. Insofar as the 18 month (+25%) 
    surveillance has proven to be acceptable, extension to a 24 month 
    (+25%) cycle is consistent with the vendor's recommendation. Any 
    additional uncertainty generated due to the extended surveillance is 
    bounded by the uncertainty inherent in a grab sample taken once per 
    24 hours which is the required compensatory action should the 
    monitor be inoperable. Since setpoints for alarms are not critical 
    to either plant operation or safety, since extensive margin is 
    reflected between the setpoint and applicable limits, it is 
    concluded that any additional uncertainty involved in a longer 
    surveillance cycle will not result in a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        This monitor measures the activity of potentially radioactive 
    gaseous effluent through the stack vent. The alarm setpoints are set 
    at a point sufficiently above expected radioactivity levels to avoid 
    unnecessary alarms and, at the same time, far below discharge 
    limits. The purpose of the monitor is to annunciate in the event an 
    unexpected spike in radioactivity level should occur so that 
    corrective action can be taken prior to exceeding a discharge limit. 
    The margin that exists between the discharge limit and the setpoint 
    is more than sufficient to accommodate any drift that could be 
    practically expected in a 24 month (+25%) operating cycle.
        In this capacity, the monitor does not have setpoints which are 
    critical to plant operation or safety. Readings are not used in a 
    quantitative manner nor is accuracy important. It is important that 
    the instrument remain operable and respond to step changes in 
    radioactivity level over the operating cycle. It is therefore 
    concluded that an extended operating cycle will not result in the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. There has been no reduction in the margin of safety.
        Sufficient margin exists between plant setpoints and applicable 
    limits to accommodate any realistic drift projected to occur over a 
    30 month operating cycle. Furthermore, instrument indications are 
    not used in a quantitative manner nor is instrument accuracy of 
    importance. Therefore, it is concluded that no significant reduction 
    in the margin of safety will result from an extended operating 
    cycle.
        (12) High Pressure Water Fire Protection System
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the system functional test of the High-
    pressure Water Fire Protection System be changed from every 18 
    months (+25%) to every 24 months (+25%).
        This system is a static system which is not normally required to 
    operate. The main fire pumps are on standby and are not in operation 
    except for testing. Thus, almost no wear is induced as a function of 
    time except that which results from being in standby status which is 
    minimal and slow acting. Under these circumstances, extending the 
    operating cycle between surveillances would be expected to have 
    negligible affect upon system operability. It is therefore concluded 
    that there would be no significant increase in the probability or 
    consequences of an accident as a result of an extended interval 
    between surveillances.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        Extension of the plant operating cycle will primarily extend the 
    time the pumps are in standby capacity. The potential for system 
    deterioration is minimal under these circumstances. Any 
    deterioration that does occur will be slow acting with respect to 
    time. A significant deterioration would be detected by a monthly 
    pump operating test. Thus, an extended operating cycle is not 
    expected to create the possibility of a new or different kind of 
    accident form [from] any previously analyzed.
        3. There has been no reduction in the margin of safety.
        Extension of the operating cycle by several months only serves 
    to extend the period of time when the pumps are in standby status. 
    Any deterioration under these circumstances will be slow acting. 
    Significant deterioration would be detected by the monthly operating 
    test. Therefore, it is concluded that an extended interval between 
    surveillances will involve no significant reduction in the margin of 
    safety.
        (13) Fire Protection System Diesel Engine
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the Fire Protection System Diesel Engine 
    Functional test be changed from every 18 months (+25%) to every 24 
    months (+25%).
        Except for periodic testing, the diesel is in a standby state 
    and not subject to operational stress. Periodic testing imposes 
    limited wear as evidenced by the absence of major repairs during 
    past maintenance. Extension of the operating cycle for several 
    months is expected to have virtually no impact upon diesel 
    operability. Monthly testing would detect any degradation. Thus it 
    is concluded that there would be no significant increase in the 
    probability or consequences of an accident as a result of an 
    extended interval between surveillances.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        Extension of the plant operating cycle will, for the most part, 
    only extend the time spent by the pumps in standby capacity. The 
    potential for system deterioration is minimal under these 
    circumstances. Any deterioration that does occur will be slow acting 
    with respect to time. Significant deterioration in performance would 
    be detected by the monthly pump operating test. Thus, an extended 
    operating cycle is not expected to create the possibility of a new 
    or different kind of accident from any previously analyzed.
        3. There has been no reduction in the margin of safety.
        Extension of the operating cycle by several months only serves 
    to extend the period of time when the pumps are in standby status. 
    Any deterioration under these circumstances will be slow acting and 
    significant deterioration would be detected by the monthly operating 
    test. Therefore, it is concluded that an extended interval between 
    surveillances will involve no significant reduction in the margin of 
    safety.
        (14) Electrical Tunnel, Diesel Generator Building, and 
    Containment Fan Cooler Fire Protection Spray Systems; (A) System 
    Functional Test and (B) Spray Header Visual Inspection
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        (a) It is proposed that the functional test surveillance 
    interval for the Electrical Tunnel, Diesel Generator Building and 
    Containment Fan Cooler Fire Protection Spray Systems be changed from 
    every 18 months (+25%) to every 24 months (25%).
        (b) It is proposed that the Spray Header visual inspection 
    interval be revised from every 18 months (25%) to 24 months (+25%).
        Extension of the surveillance interval for Electrical Tunnel and 
    Diesel Generator Building Fire Protection System functional tests 
    will have virtually no impact upon the operability of these systems. 
    These systems are accessible during normal operation and other 
    sections of the Technical Specifications (4.14.A.1.g.(i) and 
    4.14.B.1.a(i)) require that the system valve tests be conducted on 
    an annual (12 month) basis. These annual tests would reveal any 
    system deterioration prior to the conclusion of the proposed 
    extended surveillance interval.
        For the Fan Cooler Fire Protection System as well as the Spray 
    Header itself, evaluation of surveillance data from the past five 
    refueling outages indicates minor discrepancies which would not have 
    impaired system operability.
        It is therefore concluded that extension of the proposed 
    surveillance interval will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        For the Electrical Tunnel and Diesel Generator Building, 
    extension of the surveillance interval will have a negligible affect 
    as other portions of the Technical Specifications require the same 
    surveillance on an annual basis. For the spray header and the fan 
    cooler fire protection system, historical surveillance data 
    validates operability over an 18 month (+25%) interval which lends 
    confidence to conclude that operability will be maintained over a 24 
    month (+25%) interval. It is therefore concluded that the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated has not been introduced.
        3. There has been no reduction in the margin of safety.
        Extension of the surveillance for two systems will have minimal 
    impact as the Technical Specifications impose more frequent testing 
    for system valves on an annual basis. For the Spray Header and Fan 
    Cooler Fire Protection System, as well as the fire protection system 
    for the Diesel Generator Building and Electrical Tunnel, it can be 
    stated that these systems are static existing mainly in a standby 
    capacity under which little deterioration would be expected. Past 
    surveillance data validates system reliability. It is therefore 
    concluded that increasing the time interval between inspections 
    would not involve a significant reduction in the margin of safety.
        (15) Penetration Fire Barriers
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the visual inspection frequency of the 
    penetration fire barriers listed in the Technical Specifications be 
    changed from every 18 months (+25%) to every 24 months (+25%).
        The fire barrier penetration seals are static devices existing 
    in standby status. Normal environmental conditions exist during 
    normal plant operations. The only deterioration expected would be 
    that due to aging in a normal ambient which would be minimal to non-
    existent. Evaluation of unacceptable seals detected during 
    surveillances indicates that initial seal installation was faulty 
    and aging was not the cause. Surveillances during four refueling 
    outages confirm this evaluation. Accordingly, it is not expected 
    that the proposed change in surveillance interval will involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        Past surveillances indicate that time is not a predominate 
    failure mechanism. In the few unacceptable seals detected, the 
    initial installation procedure has been identified as the cause of 
    the problems. Since the seals are static devices which exist in a 
    standby condition and experience normal ambient conditions during 
    normal operation, this would be the expected conclusion. In 
    addition, the fire barriers are just one means of fire protection. 
    Other means of fire protection exist such as fire alarms, sprinklers 
    and heat detectors which provide defense in depth. Thus, it is 
    concluded that the proposed change in the surveillance interval will 
    not create the possibility of a new or different kind of accident 
    from that previously evaluated.
        3. There has been no reduction in the margin of safety.
        Aging has not been identified as a principle contributor to seal 
    failures. In addition, there exists additional means of fire 
    protection which provides defense in depth. Therefore, the proposed 
    change in surveillance intervals is not expected to involve a 
    significant reduction in the margin of safety.
        (16) Smoke Detectors/Electrical Penetration Area Inside 
    Containment
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the surveillance interval for the smoke 
    detectors located in the electrical penetration area inside 
    containment be revised from every 18 months (+25%) to every 24 
    months (+25%).
        Based on data taken from six surveillances from 1984 through and 
    including 1993, these devices have proven to be highly reliable. No 
    test failures were observed during this period. Based on the 
    guidance contained in Generic Letter 91-04, this demonstration of 
    reliable performance provides an adequate basis to conclude that the 
    proposed extension in the surveillance interval will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        Only 3 of the 5 detectors are required during normal operation. 
    Past surveillance data from six refueling outages indicate that it 
    is reasonable to expect all 5 detectors will remain operable over 
    the extended operating cycle which provides margin. It is therefore 
    concluded that the possibility of a new or different kind of 
    accident from any accident previously evaluated has not been 
    created.
        3. There has been no reduction in the margin of safety.
        The proven reliability of these devices indicates that a 
    significant reduction in the margin of safety would not be involved 
    in extending the operating cycle to 24 months (+25%).
        (17) Functional Testing of Containment Sump Pumps
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the functional test of the Containment Sump 
    Pump be changed from every 18 months (+25%) to every 24 months 
    (+25%).
        No credit is taken within the FSAR for the Containment Sump 
    Pumps as a means of mitigating the consequences of an accident. 
    During normal operation the pumps serve as a means of quantifying 
    leakage inside Containment and therefore serve a safety function in 
    terms of accident prevention. However, in this capacity they are 
    only one of several systems which are capable of serving this 
    function and their failure would not result in a loss of this 
    capability.
        In addition, evaluation of surveillance data back to 1986 
    indicates, with one exception, that the devices are very reliable. 
    In one instance, the pumps did not actuate or cause operation within 
    the setpoint tolerance but did operate as required. This was 
    determined not to be a time dependent event.
        It is therefore concluded that extending the interval between 
    refueling surveillances will not result in a significant increase in 
    the probability or consequences of an accident.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        Past surveillances indicate that time is not a predominate 
    failure mechanism. Also, there exists a Technical Specification 
    requirement to perform almost the same surveillance on a monthly 
    basis in addition to every refueling outage. This monthly test 
    diminishes any potential risk in extending the operating cycle. It 
    is therefore concluded that the possibility of a new or different 
    kind of accident from any previously analyzed has not been created.
        3. There has been no reduction in the margin of safety.
        Past surveillance data indicates that pump operation is 
    reliable. In addition, there are alternate means of providing the 
    safety function fulfilled by these pumps. Also, a monthly test is 
    required which would detect any malfunction prior to the end of an 
    extended operating cycle. It is therefore concluded that extending 
    the operating cycle by several months will not result in a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: Michael J. Case, Acting
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: November 2, 1994
        Description of amendment request: The proposed amendments will 
    upgrade existing TS 3/4.6.2.1 and TS 3/4.6.2.3 by adapting the combined 
    specification for Containment Spray and Cooling Systems, contained in 
    the Standard Technical Specifications for Combustion Engineering 
    Plants, to the St. Lucie units. The changes account for plant-specific 
    differences and include all related requirements of NUREG-1432, Rev. O, 
    specification 3.6.6A. Accordingly, the proposal is consistent with the 
    Commission's Final Policy Statement on Technical Specifications 
    Improvements (58 FR 39132).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Pursuant to 10 CFR 50.92, a determination may be made that a 
    proposed license amendment involves no significant hazards 
    consideration if operation of the facility in accordance with the 
    proposed amendment would not: (1) involve a significant increase in 
    the probability or consequences of an accident previously evaluated; 
    or (2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or (3) involve a significant 
    reduction in a margin of safety. Each standard is discussed as 
    follows:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendment will upgrade the existing Limiting 
    Conditions for Operation (LCOs) associated with the Containment 
    Cooling and Spray Systems to be consistent with NUREG-1432, Standard 
    Technical Specifications for Combustion Engineering Plants. The 
    Containment Cooling and Spray Systems are not initiators of 
    accidents previously evaluated, but are included as part of the 
    success paths associated with mitigating various accidents and 
    transients. The redundancy afforded by Containment Cooling and Spray 
    Systems in conjunction with the requirements of the proposed LCO 
    assures that the safety function of these systems can be 
    accomplished considering single failure criteria. Neither the design 
    nor the safety function of the Containment Cooling and Spray Systems 
    have been altered, and the proposed amendment does not change the 
    applicable plant safety analyses. Therefore, operation of the 
    facility in accordance with the proposed amendment will not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendment will not change the physical plant or the 
    modes of operation defined in the facility license. The changes are 
    administrative in nature in that they do not involve the addition of 
    new equipment or the modification of existing equipment, nor do they 
    otherwise alter the design of St. Lucie Unit 1 & 2 systems. 
    Therefore, operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The safety function of the Containment Cooling System is to 
    provide containment heat removal during normal operation and 
    accident conditions. The safety function of the Containment Spray 
    System is to provide containment heat and iodine removal during 
    accident conditions. The proposed amendment, in conjunction with the 
    redundancy afforded by the Containment Cooling and Spray system 
    design, assures that these safety functions can be accomplished 
    considering single-failure criteria. The bases for required actions 
    and the action completion times specified for inoperable Containment 
    Cooling and Spray trains are consistent with the corresponding 
    specifications in NUREG-1432. The safety analyses for applicable 
    accidents and transients remain unchanged from those previously 
    evaluated and reported in the Updated Final Safety Analysis Report. 
    Therefore, operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        Based on the above discussion and the supporting Evaluation of 
    Technical Specification changes, FPL has determined that the 
    proposed license amendment involves no significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: Harold F. Reis, Esquire, Newman and 
    Holtzinger, 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: Mohan Thadani, Acting
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: November 7, 1994
        Description of amendment request: The proposed amendment would 
    change the number of diesel generators (emergency power supply) 
    required to be operable during Mode 5 with the loops filled and Mode 6 
    with greater than or equal to 23 feet of water above the reactor vessel 
    flange. In addition, changes to certain system specifications that are 
    affected by the changes for the emergency power supply were also 
    proposed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of accidents previously 
    evaluated.
        The equipment which is affected by the technical specification 
    changes proposed here are not precursors to any accident postulated 
    to occur in Modes 5 and 6. Therefore, the probability of an accident 
    is not increased. A design review has demonstrated the ability of 
    the required systems to perform their accident mitigation functions 
    for the postulated accidents during Mode 5 and 6 operation. 
    Therefore, it is concluded that an increase in the consequences of 
    the postulated accidents will not result from the proposed Technical 
    Specifications.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The system design, function, and performance is not affected by 
    these specifications. No new equipment interactions are created. 
    Calculations and Failure Modes and Effects Analyses (FMEA) have been 
    conducted for selected mechanical systems and show there are no 
    failures which would cause situations where applicable accidents 
    would not be mitigated or which would cause new accidents. On this 
    basis, the proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The electrical power system specifications support the equipment 
    required to be operable, commensurate with the current level of 
    safety, including the equipment requiring a diesel backed power 
    source. The design review results demonstrate that operation in 
    Modes 5 and 6, in accordance with the proposed Technical 
    Specification changes, is acceptable from an accident mitigation 
    standpoint. The basic Modes 5 and 6 plant system functions are not 
    changed. On this basis, the proposed change does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges, Learning Center, 911 Boling Highway, Wharton, Texas 77488
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: November 7, 1994
        Description of amendment request: The proposed amendment would 
    permit both containment personnel airlock doors to be open while moving 
    fuel during refueling operations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed change involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        The proposed change to Technical Specification 3.9.4, 
    Containment Building Penetrations, would allow the containment 
    personnel airlock to be open during fuel movement and core 
    alterations. The containment personnel airlock is closed during fuel 
    movement and core alterations to prevent the escape of radioactive 
    material in the event of a fuel handling accident. The containment 
    personnel airlock is not an initiator to any accident. Whether the 
    containment personnel airlock doors are open or closed during fuel 
    movement and core alterations has no affect on the probability of 
    any accident previously evaluated.
        The proposed change does alter assumptions previously made in 
    evaluating the radiological consequences of the fuel handling 
    accident inside the reactor containment building. The proposed 
    change allows for the containment personnel airlock to be open 
    during refueling. The radiological consequences described in this 
    change are bounded by those given in the South Texas Project Safety 
    Evaluation Report and General Design Criteria 19. All doses for the 
    proposed change are less than the acceptance criteria, therefore, 
    there is no significant increase in the consequences of an accident 
    previously analyzed.
        The proposed change will significantly reduce the dose to 
    workers in the containment in the event of a fueling handling 
    accident by accelerating the containment evacuation process. The 
    proposed change will also significantly decrease the wear on the 
    containment personnel airlock doors and, consequently, increase the 
    reliability of the containment personnel airlock doors in the event 
    of an accident.
        Since the probability of a fuel handling accident is unaffected 
    by the airlock door positions, and the increased doses do not exceed 
    acceptance limits, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed change affects a previously evaluated accident, 
    e.g., a fuel handling accident inside containment. The existing 
    accident has been modified to account for the containment personnel 
    airlock doors being opened at the time of the accident. It does not 
    represent a significant change in the configuration or operation of 
    the plant and, therefore, does not create the possibility of a new 
    or different type of accident from any accident previously 
    evaluated.
        3. Does the proposed change involve a significant reduction in a 
    margin of safety?
        The margin of safety is reduced when the offsite and control 
    room doses exceed the acceptance criteria in the STP SER. As 
    previously discussed in the response to question 1, the offsite and 
    control room doses are below the acceptance criteria. Therefore, 
    this proposed change does not significantly reduce the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges, Learning Center, 911 Boling Highway, Wharton, Texas 77488
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: November 8, 1994
        Description of amendment request: The proposed amendment would 
    require only one of the two battery chargers associated with each Class 
    1E 125 VDC Channel I and Channel IV to be operable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of accidents previously 
    evaluated.
        A single charger is able to maintain the operability of Channel 
    I or Channel IV at the design loading with a single failure 
    condition. The proposed change does not alter equipment or 
    assumptions made in previously evaluated accidents. The consequences 
    of previously evaluated accidents are not increased. On this basis, 
    the proposed change does not involve a significant increase in the 
    probability or consequences of accidents previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed change involves only the operability requirement 
    for the second battery charger in Channel I and Channel IV. The 
    failure modes and operating modes would then be identical for all 
    four STPEGS Class 1E DC channels. Failure modes and effects analyses 
    already performed for DC Channels II and III would thus become 
    applicable to Channels I and IV also. The change proposed by this 
    Technical Specification revision is bounded by the failure modes and 
    effects analysis provided as Table 8.3-8 of the STPEGS UFSAR 
    [Updated Final Safety Analysis Report]. On this basis, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The proposed change involves only the operability requirement 
    for the second battery charger in Channel I and Channel IV. The 
    number and capacity of DC channels required is not affected by the 
    proposed change. The electrical loads supported by these DC channels 
    are not changed and the duration of their function is not impacted. 
    On this basis, the proposed change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges, Learning Center, 911 Boling Highway, Wharton, Texas 77488
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, NW, Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: November 8, 1994
        Description of amendment request: The proposed amendment would 
    permit the substitution of an extended range neutron flux monitor for 
    one of the source range neutron flux monitors during refueling 
    operations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident as previously 
    evaluated.
        During refueling operations, the Source Range channels are used 
    only for monitoring changes in core reactivity, and does not provide 
    inputs for automatically actuated equipment. The same function could 
    be performed by an Extended Range channel. The combination of the 
    present Channel Check and the proposed Channel Calibration are 
    sufficient to ensure that the detectors are capable of monitoring 
    core reactivity changes. By providing the intended redundant core 
    reactivity monitoring, neither the possibility or consequences of an 
    accident previously evaluated are increased.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        During refueling operations, the Source Range Monitors are used 
    simply as monitoring instrumentation. Extended Range Monitors are 
    capable of performing this function. The combination of the present 
    Channel Check and the proposed Channel Calibration are sufficient to 
    ensure that the detectors are capable of monitoring core reactivity 
    changes.
        The proposed change would require revision of STP refueling 
    procedures. However, the physical movement of fuel assemblies is 
    within the scope of current refueling procedures. No new mechanism 
    for fuel misloading or damage or boron dilution would be created by 
    the change. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change provides core reactivity monitoring 
    comparable to that provided by the use of the Source Range channels. 
    The Extended Range channel is capable of detecting core reactivity 
    changes and provides the intended redundancy. The combination of the 
    present Channel Check and the proposed Channel Calibration are 
    sufficient to ensure that the detectors are capable of monitoring 
    core reactivity changes. No margin of safety is compromised by this 
    change.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges, Learning Center, 911 Boling Highway, Wharton, Texas 77488
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine 
    YankeeAtomic Power Station, Lincoln County, Maine
    
        Date of amendment request: October 24, 1994
        Description of amendment request: The proposed amendment would 
    modify Technical Specifications Table 4.1-3 surveillance requirements 
    for new emergency feedwater flow instrumentation. Specifically, the 
    currently installed analog feedwater flow transmitters would be 
    replaced by new, digital-type flow transmitters. The new digital flow 
    emergency feedwater flow transmitters are continuously self-checking 
    and have a recommended calibration interval of 9 years. The licensee 
    proposes to verify flow whenever the system operates and send one 
    transmitter back to the manufacturer for recalibration every refueling 
    outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The staff's analysis is 
    presented below:
        1. The proposed change does not involve a significant increase in 
    the
         probability or consequences of an accident previously evaluated.
        Performance of Technical Specifications Table 4.1-3 (items 10 a and 
    b) ensures the emergency feedwater flow transmitters are operable when 
    required. The proposed change will continue to ensure operabililty and 
    therefore will not increase the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Emergency feedwater flow transmitter operability verification is 
    maintained, with no change to the system's configuration. Thus, there 
    is no unique operating condition that could adversely affect system 
    functional performance.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        There is no change to any Final Safety Analysis Report Chapter 14 
    (Safety Analysis) event. There is no change to the demonstration of 
    component operability; thus, the proposed change does not involve a 
    significant reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, Maine 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, Maine 04011
        NRC Project Director: Walter R. Butler
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: October 7, 1994
        Description of amendment request: The proposed amendment would 
    remove from the Technical Specifications certain audit responsibilities 
    of the Nuclear Safety Audit Review Committee and certain review 
    responsibilities of the Station Operation Review Committee relating to 
    the Emergency Plan and Security Plan and their implementing procedures. 
    The proposed changes are consistent with the guidance of Generic Letter 
    93-07.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 CFR 
    50.92(c)(1)) because the proposed changes do not affect the manner by 
    which the facility is operated and do not change any facility design 
    feature or equipment. Since there is no change to the facility or 
    operating procedures, there is no affect upon the probability or 
    consequences of any accident previously analyzed.
        B. The changes do not create the possibility of a new or different 
    kindof accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because they do not affect the manner by which the 
    facility is operated. The proposed changes merely affect audit and 
    review responsibilities and their deletion or relocation to other 
    controlled documents does not introduce new or different accident 
    scenarios.
        C. The changes do not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)) because the proposed changes do not 
    affect the manner by which the facility is operated or involve 
    equipment or features which affect the operational characteristics of 
    the facility.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location:  Exeter Public Library, 47 
    Front Street, Exeter, NH 03833.
        Attorney for licensee: Thomas Dignan, Esquire, Ropes & Gray, One 
    International Place, Boston, MA 02110-2624.
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company (NNECO), Docket No. 50-245, 
    Millstone Nuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of amendment request: October 14, 1994
        Description of amendment request: The proposed change clarifies the 
    low pressure coolant injection (LPCI) requirements as required by 
    Technical Specification 4.5.A.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed change in accordance with 10 CFR 
    50.92 and concluded that the change does not involve a significant 
    hazards consideration (SHC). The basis for this conclusion is that 
    the three criteria of 10 CFR 50.92(c) are not compromised. The 
    proposed change does not involve an SHC because the change would 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The LPCI flow surveillance requirement to demonstrate that three 
    pumps can deliver 15,000 gpm does not relate to any previously 
    analyzed accident. There are no accident scenarios which rely upon 
    three pumps or 15,000 gpm. The existing scenarios are more limiting 
    in that they rely on, at the most, two LPCI pumps. The actual 
    testing of the pumps in accordance with the [inservice testing] IST 
    program and Technical Specification 4.13 will not change. The 
    testing of the pumps currently performed demonstrates that LPCI will 
    function to mitigate the postulated accidents. Therefore, the 
    elimination of the requirement to demonstrate that three pumps can 
    deliver 15,000 gpm will not involve an increase in the probability 
    or consequence of any previously evaluated accident.
        The elimination of a requirement to test the LPCI header 
    instrumentation can not result in an increase to the probability or 
    consequence of an accident, since no such instrumentation exists, or 
    is required.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed change will remove a requirement to perform a 
    mathematical evaluation that provides no safety benefit. There is no 
    change in the test methodology currently performed. All four LPCI 
    pumps are tested. Deleting the requirement to verify that three LPCI 
    pumps can produce 15,000 gpm flow does not create the possibility of 
    a new or different type of accident.
        Deleting the requirement to test the LPCI spray header 
    instrumentation can not create the possibility of a new or different 
    kind of accident, since there is no LPCI header instrumentation. 
    This change corrects an error which was introduced by an earlier 
    License Amendment.
        3. Involve a significant reduction in the margin of safety.
        This change to the LPCI testing requirements does not change any 
    of the actual testing, or individual component requirements which 
    exist for the LPCI system. The change to remove the three pump, 
    15,000 gpm flow requirement eliminates the need to calculate a value 
    which provides no relevant information in ascertaining the ability 
    of the LPCI system to perform its required safety function. The 
    existing testing ensures performance of the LPCI subsystem in 
    accordance with the accident analysis requirements. The intent of 
    the Technical Specification Surveillance Requirement remains 
    unchanged. Elimination of the requirement to test the LPCI header 
    instrumentation corrects an error introduced in an earlier License 
    Amendment. No LPCI header instrumentation exists, therefore, no 
    credit was taken for such instrumentation in determining the margin 
    of safety.
        This change can not involve a significant reduction in the 
    margin of safety since there are no changes to the surveillance 
    requirements for any of the individual components of the LPCI 
    system.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: October 17, 1994, as supplemented 
    October 27, 1994
        Description of amendment requests: The proposed amendments would 
    change the submittal frequency of the Radioactive Effluent Release 
    Report from semiannual to annual in accordance with 10 CFR 50.36a.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated
        The proposed license amendments are requested to implement a 
    revision to 10 CFR 50.36a. The requested amendment[s] does not alter 
    any administrative controls over radioactive effluents, nor do they 
    affect any accident evaluations. Also, the requested amendments do 
    not involve any physical alterations to the plant with respect to 
    radioactive effluents. The proposed changes would only affect the 
    reporting requirements concerning routine data for radioactive 
    effluents.
        Therefore, the probability or consequences of an accident 
    previously evaluated are not affected by any of the proposed 
    amendments.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed
        The proposed license amendments are requested to implement a 
    revision to 10C FR 50.36a. The requested amendment[s] does not alter 
    any administrative controls over radioactive effluents, nor do they 
    involve any physical alterations to the plant with respect to 
    radioactive effluents. Also, the requested amendments do not change 
    the method by which any safety-related system performs its function. 
    The proposed changes would only affect the reporting requirements 
    concerning routine data for radioactive effluents.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be 
    created.
        3. The proposed amendment will not involve a significant 
    reduction in the margin of safety
        The proposed license amendments are requested to implement a 
    revision to 10 CFR 50.36a. The requested amendment[s] does not alter 
    any administrative controls over radioactive effluents, nor do they 
    involve any physical alterations to the plant with respect to 
    radioactive effluents. The proposed changes would only affect the 
    reporting requirements concerning routine data for radioactive 
    effluents. The operation of systems and equipment remains unchanged.
        Therefore, a significant reduction in the margin of safety would 
    not be involved.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: October 25, 1994
        Description of amendment request: The amendment would add to the 
    Susquehanna Units 1 and 2 Technical Specifications, isolation signals 
    to Table 3.6.3-1 for the containment isolation valves on the sample 
    lines for the containment radiation monitoring (CRM) and wetwell sample 
    lines. This change is based on the licensee's design change for 
    installation of a new CRM and wetwell sample system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The addition of the new CRM and Wetwell Sample System does not 
    affect any of the postulated initiating events identified in Chapter 
    6 and 15 of the FSAR, the Design Assessment Report, the current 
    Reload Analysis or the NRC Safety Evaluation Report (NUREG 0776).
        The new CRM and Wetwell Sample System with separate containment 
    sample lines is isolated from the primary containment under accident 
    conditions. The power and control-power to the CRM from the Class 1E 
    Division I and Division II sources is through electrical isolation 
    schemes so that failure(s) in the CRM under accident conditions is 
    isolated from the Class 1E systems.
        The addition of a new CRM and Wetwell Sample System with 
    separate sample lines and isolation valves does represent a change 
    in the probability of occurrence of a malfunction of equipment. The 
    addition of the auxiliary relay to the Division I and Division II 
    CAC System containment isolation logic does represent the source of 
    another potential malfunction in the logic due to the additional 
    relay in the circuit. However, the increase in probability due to 
    the additional relay is considered to be so small or insignificant 
    that the change is within the error bounds associated with the 
    original design calculations and does not constitute a significant 
    increase in probability of the overall system malfunction.
        Thus, the addition of a new CRM and Wetwell Sample System does 
    not significantly increase the probability of occurrence or the 
    consequences of an accident or malfunction of equipment important to 
    safety, as previously evaluated in the SAR.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        Chapter 6 and 15 of the FSAR, the Design Assessment Report, the 
    current Reload Analysis and NUREG-0776 were reviewed to determine if 
    the proposed action had the potential of creating a postulated 
    initiating event which was not within the spectrum of events which 
    transient or anticipated operational occurrences and accident 
    conditions were analyzed. The review did not identify a postulated 
    initiating event which would create the possibility for an accident 
    of a different type.
        A random single failure in the CRM A or CRM B does not create a 
    malfunction of a different type. A random single failure in the 
    existing containment isolation circuitry, the new isolation valve 
    control circuitry or the new valve position indication circuitry for 
    the new containment isolation valves does not create a malfunction 
    of a different type. The consequences of random single failure of 
    the CRM or the CRM and Wetwell containment isolation valve isolation 
    signal, control and indication circuitry is the same as the existing 
    consequences.
        Thus, the addition of a new CRM and Wetwell Sample System does 
    not create a possibility for an accident or malfunction of a new or 
    different type.
        3. Involve a significant reduction in a margin of safety.
        The operability of the primary containment isolation valves for 
    the sample lines to the new CRMs and Wetwell Sample Rack is governed 
    by Technical Specification Section 3/4.6.3 entitled ``Containment 
    Systems, Primary Containment Isolation Valves'' with Table 3.6.3-1 
    establishing the maximum isolation time. The bases for operability 
    of the primary containment isolation valves is to ensure that the 
    containment atmosphere is isolated from the outside environment in 
    the event of a release of radioactive material to the containment 
    atmosphere or pressurization of the containment. This is consistent 
    with GDC 54 through 57 of 10 CFR 50, Appendix A. The bases for the 
    containment isolation within the time limits specified in Table 
    3.6.3-1 is for those isolation valves designed to close 
    automatically to ensure that the release of radioactive material to 
    the environment is consistent with the assumptions used in the 
    analyses for a LOCA. The new CRM and Wetwell Sample Rack sample line 
    isolation valves are solenoid valves which close immediately on an 
    accident signal. The proposed action does not affect the operability 
    requirements of Section 3/4.6.3. The margin of safety as defined in 
    the Technical Specification for the containment isolation valves is 
    not affected.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: November 11, 1994
        Brief description of amendments: The proposed amendment would 
    modify the technical specifications (TS) by deleting accelerated 
    testing and special reporting requirements for CPSES Units 1 and 2 
    emergency diesel generators. These changes are based on Generic Letter 
    94-01, ``Removal of Accelerated Testing and Special Reporting 
    Requirements for Emergency Diesel Generators,'' dated May 31, 1994.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed change involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        Deletion of the requirement for special reporting of EDG 
    failures has no relation to probability or consequences of 
    accidents. Therefore, deletion of the requirement for special 
    reporting of EDG failures does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        There are no initiating events in accidents previously evaluated 
    that involve testing of EDGs. Therefore, deletion of accelerated 
    testing of EDGs does not involve a significant increase in the 
    probability of an accident previously evaluated.
        A reduction in the number of test starts decreases EDG component 
    stress and wear and decreases unavailability time for maintenance 
    and pre and post run checks. The resulting change in EDG reliability 
    and availability is an improvement toward ensuring the EDGs are 
    capable of fulfilling their functional requirement to provide 
    electric power for safe shutdown of the plant during loss of offsite 
    power. Furthermore, implementation of the maintenance rule 
    provisions for performance monitoring and root cause analysis for 
    failures as a basis for establishing corrective actions establish an 
    alternate reliability basis that is at least equivalent to that 
    established by accelerated testing. Therefore, deletion of 
    accelerated testing of EDGs does not involve a significant increase 
    in the consequences of an accident previously evaluated.
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        Deletion of the requirement for special reporting of EDG 
    failures introduces no new failure modes for the EDGs or other plant 
    systems and therefore has no relation to creation of accidents. 
    Therefore, deletion of the requirement for special reporting of EDG 
    failures does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The frequency at which EDG testing occurs does not affect the 
    potential failure modes of the EDGs, which have already been 
    assessed in the CPSES design. Therefore, deletion of accelerated 
    testing of EDGs does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does the proposed change involve a significant reduction in a 
    margin of safety?
        Acceptance limits and failure values are not affected by the 
    requirement for special reporting of EDG failures. Therefore, 
    deletion of the requirement for special reporting of EDG failures 
    does not involve a significant reduction in a margin of safety.
        The margin of safety impact associated with accelerated testing 
    relates to EDG reliability and availability. A reduction in the 
    number of test starts decreases EDG component stress and wear and 
    decreases unavailability time for maintenance and pre and post run 
    checks. The resulting change in EDG reliability and availability is 
    an improvement toward ensuring the EDGs are capable of fulfilling 
    their functional requirement to provide electric power for safe 
    shutdown of the plant during loss of offsite power. Furthermore, 
    implementation of the maintenance rule provisions for performance 
    monitoring and root cause analysis for failures as a basis for 
    establishing corrective actions establish an alternate reliability 
    basis that is at least equivalent to that established by accelerated 
    testing. Therefore, deletion of accelerated testing of EDGs does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019
        Attorney for licensee: George L. Edgar, Esq., Newman and 
    Holtzinger, 1615 L Street, NW., Suite 1000, Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: November 11, 1994
        Brief description of amendments: The proposed amendment would 
    provide for cycle-specific allowances to account for increases in the 
    Heat Flux Hot Channel Factor between monthly surveillances.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed change involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        The proposed changes provide for the use of cycle-specific 
    allowances to account for F2Qc(z) increases 
    between surveillances. No hardware or setpoint changes are involved; 
    therefore, the changes have no impact on the probability of 
    occurrence of any accident previously analyzed.
        The proposed changes ensure that F2Qc(z) 
    remains within its limit. Thus, the changes do not increase the 
    consequences of any accident previously analyzed.
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed changes provide for the use of a cycle-specific 
    allowances to account for F2Qc(z) increases 
    between surveillances. The proposed changes do not involve any 
    hardware or setpoint changes. Therefore the changes do not create 
    the possibility of a new or different kind of accident from any 
    accident previously analyzed.
        3. Does the proposed change involve a significant reduction in a 
    margin of safety?
        The proposed changes do not affect the failure values of any 
    system or any event acceptance criteria. Higher cycle-specific 
    allowances ensure that remains below its limit between surveillances 
    and within the bounds considered in the safety analyses. Therefore, 
    the proposed changes do not involve a reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019
        Attorney for licensee: George L. Edgar, Esq., Newman and 
    Holtzinger, 1615 L Street, NW., Suite 1000, Washington, DC 20036
        NRC Project Director: William D. Beckner
        Wisconsin Public Service Corporation, Docket No. 50-305, 
    Kewaunee Nuclear Power Plant, Kewaunee County, Wisconsin
        Date of amendment request: November 8, 1994
        Description of amendment request: The proposed amendment would 
    revise the Kewaunee Nuclear Power Plant (KNPP) Technical Specifications 
    to allow application of a voltage-based repair limit for the steam 
    generator (SG) tube support plate (TSP) intersections experiencing 
    outside diameter stress corrosion cracking (ODSCC).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        This proposed change was reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed change will not:
        1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Testing of model boiler specimens for free span tubing (no TSP 
    restraint) at room temperature conditions show burst pressures in 
    excess of 5,000 psig for indications of ODSCC with voltage 
    measurements as high as 19 volts. Burst testing performed on five 
    intersections pulled from the Kewaunee SGs with up to a 2 volt 
    indication showed measured tube burst in the range of 9,537 to 9,756 
    psig. Burst testing performed on pulled tubes from other plants with 
    up to 7.5 volt indications show burst pressures in excess of 6,300 
    psi at room temperatures. Correcting for the effects of temperature 
    on material properties and the minimum strength levels, tube burst 
    capability significantly exceeds the safety factor requirements of 
    RG 1.121.
        Tube burst criteria are inherently satisfied during normal 
    operating conditions due to the presence of the TSPS. Test data 
    indicates that tube burst cannot occur within the TSP, even for 
    tubes with through wall EDM notches 0.75 inch long, when the notch 
    is adjacent to the TSP. Since tube burst is precluded during normal 
    operating conditions, the criterion that must be satisfied to 
    demonstrate adequate tube integrity is a safety margin of 1.43 times 
    MSLB pressure differential. From Figure 3-2 of EPRI report TR-
    100407, the BOC structural limit for 7/8 inch diameter tubing is 9.6 
    volts. Applying an allowance of 20% for NDE uncertainty and 50% for 
    crack growth rate over an operating cycle results in a voltage 
    repair limit of 5.6 volts. The proposed repair limit of 2 volts is 
    very conservative when compared to the 5.6 volts taking into account 
    the low average growth rates experienced at Kewaunee and the high 
    tube burst pressures.
        Relative to the expected leakage during accident condition 
    loadings, a plant specific calculation was performed to determine 
    the maximum primary-to-secondary leakage during a postulated MSLB 
    event. The evaluation considered both pre-accident and accident 
    initiated iodine spikes. The results of the evaluation show that the 
    accident spike yielded the limiting leak rate. This case was based 
    on a 30 rem thyroid dose at the site boundary and initial primary 
    and secondary coolant activity levels of 1.0 uCi/gm and 0.1 uCi/gm 
    dose equivalent iodine-131, respectively. A leak rate of 34.0 gpm 
    was determined to be the upper limit for allowable primary to 
    secondary leakage in the SG in the faulted loop. The SG in the 
    intact loop was assumed to leak at a rate of 0.1 gpm (150 gpd).
        Application of the voltage-based repair limit will be 
    supplemented with a projected EOC MSLB leakage calculation and 
    conditional burst probability assessment. The methodology for 
    performing these calculations will be consistent with that discussed 
    in the draft GL until final guidance is published. Should the 
    projected MSLB leakage be exceeded indications will be repaired or 
    removed from service until the projected leakage is less than or 
    equal to 34.0 gpm.
        Application of the voltage-based repair limit will not adversely 
    affect SG tube integrity. Therefore, the proposed amendment will not 
    increase the probability or consequences of an accident previously 
    evaluated.
        2) Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Implementation of the proposed voltage-based repair limit will 
    not reduce the overall safety or functional requirements of the SG 
    tube bundles. The tube burst criteria will be satisfied during 
    normal operating conditions by the presence of the TSPs. The RG 
    1.121 criteria that must be satisfied during accident loading 
    conditions is 1.43 times MSLB differential pressure. Conservatively, 
    the existing data base of burst testing shows that the tube burst 
    margins can be satisfied with bobbin coil signal amplitudes of about 
    8.82 volts or less regardless of the depth of tube wall penetration.
        The proposed repair criteria will be supplemented with a reduced 
    operating leakage requirement of 150 gpd average through either SG 
    to preclude the potential for excessive leakage during operating 
    conditions. The 150 gpd restriction will provide for timely leakage 
    detection and plant shutdown in the event of the occurrence of an 
    unexpected single crack resulting in leakage that is associated with 
    the longest permissible crack length. The operating leakage limit is 
    based on leak-before break considerations, critical crack length and 
    predicted leakage.
        The SG tube integrity will continue to be maintained through 
    inservice inspections and primary-to-secondary leakage monitoring. 
    Therefore, the proposed change will not create the possibility of a 
    new or different kind of accident.
        3) Involve a significant reduction in the margin of safety.
        Application of the voltage-based repair criteria has been 
    demonstrated to maintain tube integrity commensurate with the RG 
    1.121 criteria. RG 1.121 describes a method acceptable to the staff 
    for meeting GDCs 2, 14, 15, 31 and 32. This is accomplished by 
    determining the limiting degradation of SG tubing as established by 
    inservice inspection, beyond which tubes should be removed from 
    service. Upon implementation of the repair criteria, even under the 
    worst case conditions, the occurrence of ODSCC at the TSPs is not 
    expected to lead to a SG tube rupture event during normal or faulted 
    conditions. The most limiting event would be a potential increase in 
    leakage during a MSLB event. Excessive leakage during a MSLB is 
    precluded by verifying that the expected EOC crack distribution of 
    ODSCC indications at TSP locations would result in an acceptably low 
    primary-to-secondary leakage. Therefore, the radiological 
    consequences from tubes remaining in service is a small fraction of 
    the 10 CFR 100 limits.
        The combined effects of a LOCA plus SSE on the SGs were assessed 
    as required by GDC 2. This issue was addressed for the Kewaunee SGs 
    through the application of leak-before-break (LBB) principles to the 
    primary loop piping. Based on the results of this analysis, it is 
    concluded that the LBB is applicable to the Kewaunee primary loops 
    and, thus, the probability of breaks in the primary loop piping is 
    sufficiently low that they need not be considered in the structural 
    design basis of the plant. Excluding breaks in the primary loops, 
    the LOCA loads from the large branch lines were also assessed and 
    found to be of insufficient magnitude to result in SG tube collapse. 
    Based on these analysis results, no tubes are expected to collapse 
    or deform to the degree that secondary-to-primary in-leakage would 
    be increased over currently expected levels. On this basis no tubes 
    need to be excluded from the voltage-based repair criteria for 
    reasons of deformation resulting from combined LOCA and SSE 
    loadings.
        Addressing the RG 1.83 considerations, implementation of the 
    voltage-based repair criteria will include a 100% bobbin coil probe 
    inspection of all TSP intersections with known ODSCC down to the 
    lowest cold leg TSP identified. This will be supplemented by a 
    reduced operating leakage limit, enhanced eddy current data analysis 
    guidelines, MRPC inspection requirements and a projected EOC voltage 
    distribution. It is concluded that the proposed change will not 
    result in a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: Leif J. Norrholm
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: August 8, 1994
        Brief description of amendment request: The proposed amendment 
    would modify Technical Specification (TS) 4.0.5.a. to delete the 
    requirement to obtain prior written relief from the NRC for inservice 
    inspection (ISI) and inservice testing (IST) of components conducted 
    pursuant to 10 CFR 50.55a. This change would provide relief from the 
    ASME Code requirement in the interim between the submittal of a relief 
    request and the NRC's issuance of a safety evaluation regarding the 
    relief request. The change would allow the plant to operate in 
    accordance with a proposed relief request while the NRC staff completed 
    its review of the relief request. The licensee has also proposed to 
    modify TS 4.0.5.b. to add a definition for biennial or every-2-year 
    inspection and testing activities. The definition of biennial or every 
    2 years will be at least once per 731 days.Date of individual notice in 
    Federal Register: November 14, 1994 (59 FR 56558)
        Expiration date of individual notice: December 14, 1994
        Local Public Document Room location:  Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    SteamElectric Plant, Unit No. 2, Darlington County, South 
    CarolinaDate of application for amendment: June 29, 1994
    
        Brief description of amendment: The amendment deletes the 
    requirement to perform alternate train testing to demonstrate that 
    other, similar, safety-related components are operable when components 
    are found, or made, inoperable in the safety injection, residual heat 
    removal, and containment spray systems. The surveillance requirements, 
    which the licensee refers to as accelerated testing requirements, 
    affect the safety injection (SI) pumps, residual heat removal (RHR) 
    pumps, containment spray (CS), SI, RHR and CS flow paths.
        Date of issuance: November 21, 1994
        Effective date: November 21, 1994
        Amendment No. 153
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39581) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 21, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College, Hartsville, South Carolina 29550
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: June 29, 1992, as supplemented 
    February 22, 1994
        Brief description of amendment: The amendment revised TS Sections 
    3/4.3, ``Instrumentation,'' 3/4.4.2, ``Safety/Relief Valves,'' and 
    associated Bases to increase the surveillance test intervals and 
    allowable out-of-service times for specific safety-related 
    instrumentation.
        Date of issuance: November 22, 1994
        Effective date: November 22, 1994
        Amendment No. 67
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17605) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 22, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois; 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power 
    Station,Units 1 and 2, Rock Island County, IllinoisDate of 
    application for amendments: October 15, 1992
    
        Brief description of amendments: The proposed amendments would 
    revise the Dresden and Quad Cities Technical Specification (TS) 3/4.4 
    to revise the sodium pentaborate solution concentrations for the 
    Standby Liquid Control System (SLCS) storage tanks based on net 
    positive suction head test results.
        Date of issuance: November 16, 1994
        Effective date: November 16, 1994
        Amendment Nos.: 130, 124, 151, and 147
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29, and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 9, 1992 (57 FR 
    58245) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 16, 1994. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: For Dresden, The Morris Public 
    Library, 604 Liberty Street, Morris, Illinois 60450; For Quad Cities, 
    The Dixon Public Library, 221 Hennepin Avenue, Dixon, Illinois 61021.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: October 29, 1993, as 
    supplemented on March 28, 1994, and November 8, 1994.
        Brief description of amendment: The amendment revises the 
    surveillance intervals for the Volume Control Tank Level Instrument, 
    the Containment High Range Radiation Monitors, the Safety Injection 
    System Electrical Loading, the Safety Injection System, and the Reactor 
    Coolant System Subcooling Margin Monitors to accommodate a 24-month 
    fuel cycle. These revisions are being made in accordance wih the 
    guidance provided by Generic Letter 91-04, ``Changes in Technical 
    Specification Surveillance Intervals to Accommodate a 24-Month Fuel 
    Cycle.''
        Date of issuance: November 16, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 178
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37067) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 16, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: August 25, 1994
        Brief description of amendments: The amendments revise the testing 
    interval for auxiliary feedwater (AFW) system pumps from monthly to 
    quarterly on a staggered test basis. The amendments are consistent with 
    the guidance in NUREG-1366, ``Improvements to Technical Specifications 
    Surveillance Requirements'' and Generic Letter 93-05, ``Line-Item 
    Technical Specifications Improvements to Reduce Surveillance 
    Requirements for Testing During Power Operation.'' In addition, a note 
    is incorporated from NUREG-1431, ``Revised Standard Technical 
    Specifications, Westinghouse Plants'' into the TS clarifying that the 
    turbine-driven AFW pump cannot be tested until the required pressure 
    exists in the secondary side of the steam generator.
        Date of issuance: November 9, 1994
        Effective date: November 9, 1994
        Amendment Nos.: 151 and 133
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49426) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated November 9, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Florida Power and Light Company, Docket No. 50-335, St. Lucie 
    Plant, Unit No. 1, St. Lucie County, Florida
    
        Date of application for amendment: March 19, 1993, augmented August 
    18, 1994.
        Brief description of amendment: This amendment allows a reduction 
    in Reactor Coolant System design flowrate from the current value of 
    370,000 gpm to 355,000 gpm in Technical Specifications Figure 2.1-1 and 
    Tables 2.2-1 and 3.2-1.
    
        Date of issuance: November 25, 1994
        Effective date: November 25, 1994
        Amendment No.: 130
        Facility Operating License No. DPR-67: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1993 (58 FR 
    25855) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 25, 1994. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: April 29, 1994, as supplemented by 
    letter dated September 8, 1994.
        Brief description of amendments: The amendments revise the 
    technical specifications to permit revision of the maximum allowable 
    power range neutron flux high setpoint when one or more main steam 
    safety valves are inoperable. In addition, new algorithm used to 
    calculate the revised setpoint values is incorporated into the Bases 
    for the technical specifications.
        Date of issuance: November 22, 1994
        Effective date: To be implemented within 30 days of issuance
        Amendment Nos.: Unit 1 - Amendment No. 66; Unit 2 - Amendment No. 
    55
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29628) The additional information contained in the supplemental letter 
    dated September 8, 1994, was clarifying in nature and, thus, within the 
    scope of the initial notice and did not affect the staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated November 22, 1994.No significant hazards consideration 
    comments received: No
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy 
    Center,Linn County, Iowa
    
        Date of applications for amendment: June 4, 1993, as supplemented 
    February 4, 1994, and May 6, 1994.
        Brief description of amendment: The amendment revised the Technical 
    Specifications (TS) by changing the requirements of the TS Section 3.6, 
    ``Primary Systems Boundary,'' adding definitions into Section 1.0, 
    ``Definitions,'' and revising Bases Section 3/4.6. These changes 
    improved clarity and provided consistency of the TS with the Standard 
    TS (NUREG-1202). Typographical and administrative corrections were also 
    made in Section 3.6.
        Date of issuance: November 17, 1994
        Effective date: November 17, 1994, and to be implemented within 120 
    days
        Amendment No.: 203
        Facility Operating License No. DPR-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 21, 1993 (58 FR 
    39052). The May 6, 1994, application, repeated a TS change included in 
    the June 4, 1993, application, and proposed changes to the TS Bases. 
    The information in the February 14, 1994, supplement, did not change 
    theinitial no significant hazards determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated November 17, 1994. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, Iowa 52401.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of application for amendment: July 12, 1994
        Brief description of amendment: The proposed amendment changes the 
    requirement to perform the surveillance test for the channel functional 
    test Rod Block Monitor, Flow-biased Average Power Range Monitor and 
    Recirculation Flow instruments from within 24 hours prior to startup to 
    after the reactor is in the RUN mode, but prior to when each system is 
    assumed to function in the plant safety analysis.
        Date of issuance: November 18, 1994
        Effective date: November 18, 1994, to be implemented within 30 days 
    of issuance
        Amendment No.: 204
        Facility Operating License No. DPR-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45025) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 18, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, Iowa 52401
    
    South Carolina Electric & Gas Company, South Carolina Public 
    ServiceAuthority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: October 29, 1993, as 
    supplemented March 11, 1994, May 18, 1994, September 20, 1994, and 
    October 20, 1994
        Brief description of amendment: The proposed changes support the 
    installation of new steam generators at Summer Station. The changes 
    involve:
        (1) alterations to the core operating limits
        (2) changes to various reactor trip setpoints
        (3) deletion of the negative flux rate trip
        (4) removal of references to specific correlations used in the 
    departure from nucleate boiling (DNB) analyses
        (5) changes to the steam/feedwater flow mismatch activation 
    specification
        (6) changes to shutdown limits
        (7) changes to instrument uncertainty allowances
        (8) a change to the methodology for reactor coolant system (RCS) 
    flow determination
        (9) modifications to DNB parameters
        (10) a change to the engineered safety features actuation system 
    setpoints for steam generator water levels
        (11) removal of the F* and L* criteria (12) addition of a 
    requirement for a first inservice inspection for the new steam 
    generators
        Date of issuance: November 18, 1994
        Effective date: November 18, 1994
        Amendment No.: 119
        Facility Operating License No. NPF-12. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7968) The May 18, 1994, September 20, 1994, and October 20, 1994 
    submittals contained explanatory information and did not change finding 
    of nos significant hazards consideration as published in the FEDERAL 
    REGISTER. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 18, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    South Carolina Electric & Gas Company, South Carolina Public 
    ServiceAuthority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: July 20, 1994
        Brief description of amendment: The amendment changes the Technical 
    Specifications (TS) to modify TS Table 2.2-1, Reactor Trip System 
    Instrumentation Setpoints, and Table 3.3-4, Engineered Safety Features 
    Actuation System Instrumentation Trip Setpoints and several associated 
    bases. The change would remove specific rack and sensor allowable drift 
    values by removing three columns from the tables.
        Date of issuance: November 18, 1994
        Effective date: November 18, 1994
        Amendment No.: 120
        Facility Operating License No. NPF-12. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 19, 1994 (59 
    FR 47181) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 18, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: March 5, 1993, as supplemented 
    by letter dated September 22, 1994
        Brief description of amendments: These amendments propose to revise 
    Technical Specification (TS) 3/4.7.1.1, ``Main Steam Safety Valves,'' 
    and the associated Bases to (1) increase the as-found setpoint 
    tolerance of Table 3.7-1 for the Main Steam Safety Valves (MSSVs) from 
    +/- 1 percent to +2 percent and -3 percent; (2) add a footnote to Table 
    3.7-1 to indicate that the setpoint tolerance for the lowest set pair 
    of MSSVs will be +1 percent and -3 percent; (3) add a footnote to TS 
    3.7.1.1 and revise footnote 1 of Table 3.7-1 to clarify that the MSSVs 
    will be left at the lift setting according to Table 3.7-1 within a +/-1 
    percent tolerance following inservice testing; (4) add an ACTION 
    statement requiring the plant to be in HOT STANDBY within 6 hours and 
    in HOT SHUTDOWN within the following 12 hours for the case of less than 
    five MSSVs operable per operable steam generator; (5) require the plant 
    to be in ``HOT SHUTDOWN within the following 12 hours'' instead of 
    ``COLD SHUTDOWN within the following 30 hours'' per the existing ACTION 
    statement; (6) revise the title of column 1 of Table 3.7-2 to read 
    ``Number of Operable Safety Valves per Operable Steam Generator,'' 
    instead of ``Maximum Number of Inoperable Safety Valves on Any 
    Operating Steam Generator, for better readability; and (7) delete the 
    ORIFICE SIZE column of Table 3.7-1.
        Date of issuance: November 23, 1994
        Effective date: As of the date of its issuance and must be fully 
    implemented no later than 30 days from the date of issuance.
        Amendment Nos.: 114 and 103
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34093) The additional information contained in the supplemental letter 
    dated September 22, 1994, served to clarify the amendments, was within 
    the scope of the initial notice, and did not affect the Commission's 
    proposed no significant hazards consideration determination.The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated November 23, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: September 9, 1994 (TS 94-08)
        Brief description of amendments: The amendments add the main steam 
    valve vaults to the exclusion areas where containment penetration 
    integrity is not required to be verified once every 31 days for 
    penetrations that are secured in the closed position.
        Date of issuance: November 22, 1994
        Effective date: November 22, 1994
        Amendment Nos.: 191 and 183
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: October 12, 1994 (59 FR 
    51630) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 22, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
    
        Date of application for amendments: July 14, 1994
        Brief description of amendments: These amendments modify the 
    current Technical Specifications having cycle-specific parameter limits 
    in the Core Operating Limits Report.
        Date of issuance: November 15, 1994
        Effective date: November 15, 1994Amendment Nos. 194 and 194
        Facility Operating Licen se Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 12, 1994 (59 FR 
    51630) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 15, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    NuclearPower Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: May 17, 1994
        Brief description of amendment: The amendment revises the TS by 
    separating the specification for the Internal Containment Spray (ICS) 
    and the Spray Additive Systems into two distinct specifications. The 
    amendment also removes the requirement that for a spray train to be 
    operable, a spray pump suction flow path from the additive tank is 
    needed. In addition, the allowable out-of-service time for the Spray 
    Additive System is increased from 48 hours to 72 hours.
        Date of issuance: November 18, 1994
        Effective date: November 18, 1994
        Amendment No.: 113
        Facility Operating License No. DPR-43. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37090) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated November 18, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Dated at Rockville, Maryland, this 30th day of November 1994.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects - III/IV,Office of Nuclear 
    Reactor Regulation
    [FR Doc. 94-29925 Filed 12-6-94; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
12/07/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-29925
Dates:
November 21, 1994
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: December 7, 1994