[Federal Register Volume 62, Number 29 (Wednesday, February 12, 1997)]
[Notices]
[Pages 6566-6587]
From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
[FR Doc No: X97-20212]
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NUCLEAR REGULATORY COMMISSION
Biweekly Notice
Applications and Amendments to Facility Operating Licenses
Involving No Significant Hazards Considerations
I. Background
Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory
Commission (the Commission or NRC staff) is
[[Page 6567]]
publishing this regular biweekly notice. Public Law 97-415 revised
section 189 of the Atomic Energy Act of 1954, as amended (the Act), to
require the Commission to publish notice of any amendments issued, or
proposed to be issued, under a new provision of section 189 of the Act.
This provision grants the Commission the authority to issue and make
immediately effective any amendment to an operating license upon a
determination by the Commission that such amendment involves no
significant hazards consideration, notwithstanding the pendency before
the Commission of a request for a hearing from any person.
This biweekly notice includes all notices of amendments issued, or
proposed to be issued from January 17, 1997, through January 31, 1997.
The last biweekly notice was published on January 29, 1997 (62 FR
4341).
Notice Of Consideration Of Issuance Of Amendments To Facility
Operating Licenses, Proposed No Significant Hazards Consideration
Determination, And Opportunity For A Hearing
The Commission has made a proposed determination that the following
amendment requests involve no significant hazards consideration. Under
the Commission's regulations in 10 CFR 50.92, this means that operation
of the facility in accordance with the proposed amendment would not (1)
involve a significant increase in the probability or consequences of an
accident previously evaluated; or (2) create the possibility of a new
or different kind of accident from any accident previously evaluated;
or (3) involve a significant reduction in a margin of safety. The basis
for this proposed determination for each amendment request is shown
below.
The Commission is seeking public comments on this proposed
determination. Any comments received within 30 days after the date of
publication of this notice will be considered in making any final
determination.
Normally, the Commission will not issue the amendment until the
expiration of the 30-day notice period. However, should circumstances
change during the notice period such that failure to act in a timely
way would result, for example, in derating or shutdown of the facility,
the Commission may issue the license amendment before the expiration of
the 30-day notice period, provided that its final determination is that
the amendment involves no significant hazards consideration. The final
determination will consider all public and State comments received
before action is taken. Should the Commission take this action, it will
publish in the Federal Register a notice of issuance and provide for
opportunity for a hearing after issuance. The Commission expects that
the need to take this action will occur very infrequently.
Written comments may be submitted by mail to the Chief, Rules
Review and Directives Branch, Division of Freedom of Information and
Publications Services, Office of Administration, U.S. Nuclear
Regulatory Commission, Washington, DC 20555-0001, and should cite the
publication date and page number of this Federal Register notice.
Written comments may also be delivered to Room 6D22, Two White Flint
North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15
p.m. Federal workdays. Copies of written comments received may be
examined at the NRC Public Document Room, the Gelman Building, 2120 L
Street, NW., Washington, DC. The filing of requests for a hearing and
petitions for leave to intervene is discussed below.
By March 14, 1997, the licensee may file a request for a hearing
with respect to issuance of the amendment to the subject facility
operating license and any person whose interest may be affected by this
proceeding and who wishes to participate as a party in the proceeding
must file a written request for a hearing and a petition for leave to
intervene. Requests for a hearing and a petition for leave to intervene
shall be filed in accordance with the Commission's ``Rules of Practice
for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested
persons should consult a current copy of 10 CFR 2.714 which is
available at the Commission's Public Document Room, the Gelman
Building, 2120 L Street, NW., Washington, DC and at the local public
document room for the particular facility involved. If a request for a
hearing or petition for leave to intervene is filed by the above date,
the Commission or an Atomic Safety and Licensing Board, designated by
the Commission or by the Chairman of the Atomic Safety and Licensing
Board Panel, will rule on the request and/or petition; and the
Secretary or the designated Atomic Safety and Licensing Board will
issue a notice of a hearing or an appropriate order.
As required by 10 CFR 2.714, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following factors: (1) the nature of the petitioner's right under the
Act to be made a party to the proceeding; (2) the nature and extent of
the petitioner's property, financial, or other interest in the
proceeding; and (3) the possible effect of any order which may be
entered in the proceeding on the petitioner's interest. The petition
should also identify the specific aspect(s) of the subject matter of
the proceeding as to which petitioner wishes to intervene. Any person
who has filed a petition for leave to intervene or who has been
admitted as a party may amend the petition without requesting leave of
the Board up to 15 days prior to the first prehearing conference
scheduled in the proceeding, but such an amended petition must satisfy
the specificity requirements described above.
Not later than 15 days prior to the first prehearing conference
scheduled in the proceeding, a petitioner shall file a supplement to
the petition to intervene which must include a list of the contentions
which are sought to be litigated in the matter. Each contention must
consist of a specific statement of the issue of law or fact to be
raised or controverted. In addition, the petitioner shall provide a
brief explanation of the bases of the contention and a concise
statement of the alleged facts or expert opinion which support the
contention and on which the petitioner intends to rely in proving the
contention at the hearing. The petitioner must also provide references
to those specific sources and documents of which the petitioner is
aware and on which the petitioner intends to rely to establish those
facts or expert opinion. Petitioner must provide sufficient information
to show that a genuine dispute exists with the applicant on a material
issue of law or fact. Contentions shall be limited to matters within
the scope of the amendment under consideration. The contention must be
one which, if proven, would entitle the petitioner to relief. A
petitioner who fails to file such a supplement which satisfies these
requirements with respect to at least one contention will not be
permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing, including the opportunity to present evidence and cross-
examine witnesses.
If a hearing is requested, the Commission will make a final
determination on the issue of no
[[Page 6568]]
significant hazards consideration. The final determination will serve
to decide when the hearing is held.
If the final determination is that the amendment request involves
no significant hazards consideration, the Commission may issue the
amendment and make it immediately effective, notwithstanding the
request for a hearing. Any hearing held would take place after issuance
of the amendment.
If the final determination is that the amendment request involves a
significant hazards consideration, any hearing held would take place
before the issuance of any amendment.
A request for a hearing or a petition for leave to intervene must
be filed with the Secretary of the Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001, Attention: Docketing and
Services Branch, or may be delivered to the Commission's Public
Document Room, the Gelman Building, 2120 L Street, NW., Washington DC,
by the above date. Where petitions are filed during the last 10 days of
the notice period, it is requested that the petitioner promptly so
inform the Commission by a toll-free telephone call to Western Union at
1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union
operator should be given Datagram Identification Number N1023 and the
following message addressed to (Project Director): petitioner's name
and telephone number, date petition was mailed, plant name, and
publication date and page number of this Federal Register notice. A
copy of the petition should also be sent to the Office of the General
Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001,
and to the attorney for the licensee.
Nontimely filings of petitions for leave to intervene, amended
petitions, supplemental petitions and/or requests for a hearing will
not be entertained absent a determination by the Commission, the
presiding officer or the Atomic Safety and Licensing Board that the
petition and/or request should be granted based upon a balancing of
factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
For further details with respect to this action, see the
application for amendment which is available for public inspection at
the Commission's Public Document Room, the Gelman Building, 2120 L
Street, NW., Washington, DC, and at the local public document room for
the particular facility involved.
Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power
Station, Plymouth County, Massachusetts
Date of amendment request: November 26, 1996
Description of amendment request: The proposed amendment would
change the definition of ``Primary Containment Integrity,'' Note 6 on
Table 3.2.A, correct a typographical error on Table 3.2 D, correct
Table 3.2.F to reflect modifications to the plant and changes to Bases
sections 3/4.6G and 3/4.7.A. These changes are considered
administrative and have no effect on plant design, safety limit
settings or plant system operation.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
. The proposed amendment does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The proposed administrative changes involving typographical
errors, additions for clarity and consistency, and updating the
Bases do not affect plant design, safety limit settings, or plant
system operation and, therefore, do not modify or add any initiating
parameters that would significantly increase the probability or
consequences of any previously analyzed accident.
The changes to instrument numbers and type do not change the
parameters being surveyed or the number of operable channels for
these parameters. These changes do not modify or add any initiating
parameters and do not affect plant design, safety limit settings, or
plant system operation. Therefore, these instrument changes do not
involve a significant increase in the probability or consequences of
an accident previously evaluated.
2. The proposed amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
These proposed changes do not involve any potential initiating
events that would create any new or different kind of accident.
Therefore, the proposed changes do not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
3. The proposed amendment does not involve a significant
reduction in a margin of safety.
These changes do not affect any safety analysis assumptions,
system operation, structures, potential initiating events or safety
limits. Therefore, it is concluded that the proposed amendment does
not involve a significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Plymouth Public Library, 11
North Street, Plymouth, Massachusetts 02360.
Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company,
800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
NRC Project Director: Patrick D. Milano, Acting
Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power
Station, Plymouth County, Massachusetts
Date of amendment request: January 24, 1997
Description of amendment request: The proposed amendment will
update the Safety Limit Minimum Critical Power Ratio (SLMCPR) in
Technical Specification (TS) 2.1.2 and the associated Bases section to
reflect the results of the latest cycle-specific calculation performed
for the Pilgrim Nuclear Power Station Operating Cycle 12. In addition,
the values provided in Note 5 of Table 3.2.C.1, which are based on the
SLMCPR values, have been revised as a result of the changes to the
SLMCPR value.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below: 11.The proposed technical specification changes do not involve a
significant increase in the probability of an accident previously
evaluated.
The derivation of the revised SLMCPR for Pilgrim for
incorporation into the TS, and its use to determine cycle-specific
thermal limits, have been performed using NRC approved methods.
Additionally, interim implementing procedures that incorporate
cycle-specific parameters have been used which result in a more
restrictive value for SLMCPR. These calculations do not change the
method of operating the plant and have no effect on the probability
of an accident initiating event or transient.
The basis of the MCPR [minimum critical power ratio] Safety
Limit is to ensure no mechanistic fuel damage is calculated to occur
if the limit is not violated. The new SLMCPR preserves the existing
margin to transition boiling, and the probability of fuel damage is
not increased.
The basis of the MCPR criteria that define a limiting rod
pattern is to ensure the SLMCPR is not violated in the event a
control rod is fully withdrawn from the core. The new MCPR criteria
that define a limiting rod pattern continue to ensure the SLMCPR is
not violated in the event a control rod is fully withdrawn from the
core. These new criteria do not change the method of operating the
plant and have no effect on the probability of an accident
initiating event or a transient.
[[Page 6569]]
Therefore, the proposed changes do not involve an increase in
the probability or consequences of an accident previously evaluated.
2. The proposed TS changes do not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
The proposed changes result only from a revised method of
analysis for the Cycle 12 core reload. These changes do not involve
any new method for operating the facility and do not involve any
facility modifications. No new initiating events or transients
result from these changes. Therefore, the proposed TS changes do not
create the possibility of a new or different kind of accident from
any accident previously evaluated.
3. The proposed TS changes do not involve a significant
reduction in a margin of safety.
The margin of safety as defined in the TS bases will remain the
same. The new SLMCPR is calculated using NRC approved methods which
are in accordance with the current fuel design and licensing
criteria. Additionally, interim implementing procedures, which
incorporate cycle-specific parameters, have been used. The SLMCPR
remains high enough to ensure that greater than 99.9% of all fuel
rods in the core will avoid transition boiling if the limit is not
violated, thereby preserving the fuel cladding integrity.
The new MCPR criteria that define a limiting rod pattern
continue to ensure the SLMCPR is not violated in the event a control
rod is fully withdrawn from the core.
Therefore, the proposed TS changes do not involve a reduction in
the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Plymouth Public Library, 11
North Street, Plymouth, Massachusetts 02360.
Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company,
800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
NRC Project Director: Patrick D. Milano, Acting
Carolina Power & Light Company, et al., Docket No. 50-400, Shearon
Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties,
North Carolina
Date of amendment request: January 29, 1997
Description of amendment request: The proposed change adds a new
entry 3.0.5 to the plant Technical Specifications (TS) to provide
specific guidance for returning equipment to service under
administrative control for the sole purpose of performing testing to
demonstrate operability.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. The proposed amendment does not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
The proposed change does not affect the operation or design of
the plant in any way. Operation of plant equipment under this change
will not differ in any way from its normal operational mode. The
normal operation of plant equipment is not a precursor to any
accident. The purpose of tests performed using this change are to
demonstrate that required automatic actions are carried out.
Equipment will be operated under administrative control for only a
short period of time. Personnel will be immediately available to
take appropriate manual action if it should be required. Therefore
operation of equipment under this change is not expected to increase
the probability or consequences of an accident previously evaluated.
2. The proposed amendment does not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
The proposed testing allowance does not involve any physical
alterations or additions to plant equipment or alter the manner in
which any safety-related system performs its function. Therefore,
the proposed changes do not create the possibility of a new or
different kind of accident from any accident previously evaluated.
3.
The proposed amendment does not involve a signifcant reduction in
the margin of safety.
Equipment will be operated under administrative control for only
a short period of time. Personnel will be immediately available to
take appropriate manual action if it should be required. The purpose
of the testing is to restore required equipment to an OPERABLE state
which increases the automatic protection available and reduces the
reliance on the compensatory measures provided by ACTION statements.
Therefore, the proposed changes do not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Cameron Village Regional
Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
Attorney for licensee: William D. Johnson, Vice President and
Senior Counsel, Carolina Power & Light Company, Post Office Box 1551,
Raleigh, North Carolina 27602
NRC Project Director: Mark Reinhart, Acting
The Cleveland Electric Illuminating Company, Centerior Service
Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania
Power Company, Toledo Edison Company, Docket No. 50-440, Perry
Nuclear Power Plant, Unit No. 1, Lake County, Ohio
Date of amendment request: October 24, 1996
Description of amendment request: The proposed amendment to the
Perry Nuclear Power Plant Technical Specifications revises those
specifications associated with the Minimum Critical Power Ratio (MCPR)
Reactor Core Safety Limit. The revision would increase the MCPR Safety
Limit values to make them more conservative.
Basis for proposed no significant hazards determination: The NRC
staff provides its analysis of the issue of no significant hazards
consideration below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
There is no change to any plant equipment, and increasing the
MCPR Safety Limit is more conservative. Therefore, the proposed
change does not significantly increase the probability or
consequences of any accident previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
There are no physical changes to the plant, and increasing the MCPR
Safety Limit is more conservative. Therefore, the proposed changes do
not create the possibility of a new or different kind of accident from
any previously evaluated.
3. The proposed change does not involve a significant reduction
in a margin of safety.
The proposed MCPR Safety Limit values are more conservative, and
were calculated using NRC approved methods. Therefore, the proposed
change does not involve a significant reduction in a margin of safety.
The staff has reviewed the amendment request and the licensee's no
significant hazards consideration determination. Based on the review
and the above discussions, the staff proposes to determine that the
proposed changes do not involve a significant hazards consideration.
Local Public Document Room location: Perry Public Library, 3753
Main Street, Perry, Ohio 44081
Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts &
Trowbridge, 2300 N Street, NW., Washington, DC 20037
NRC Project Director: Gail H. Marcus
[[Page 6570]]
Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455,
Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos.
STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2,
Will County, Illinois
Date of amendment request: August 19, 1996
Description of amendment request: The proposed amendments revise
the steam generator (SG) repair criteria in the Byron, Unit 1, and
Braidwood, Unit 1, Technical Specifications (TS). These revisions, if
approved, would continue the use of the voltage-based SG tube repair
criteria added by Amendment No. 77, dated November 9, 1995, to the
Byron 1 TSs and by Amendment No. 69, dated November 9, 1995, to the
Braidwood 1 TSs. The subject voltage-based repair criteria are
applicable only for a specific form of SG tube degradation identified
as outer diameter stress corrosion cracking (ODSCC), which is confined
entirely within the thickness of the SG tube support plates (TSPs).
Specifically, the pending amendments for both units would continue for
one more operating cycle, the present use of a lower voltage repair
limit of 3.0 volts on the hot leg side of the SGs using the Locked-Tube
model. The cold leg side of the SGs and certain hot leg side tube/TSP
intersections (e.g., dented SG tube intersections) would continue to be
repaired using the Free-Span model. The proposed amendments are needed
because the applicability of the revised voltage-based SG tube repair
criteria for ODSCC which were added in the prior amendments cited
above, was limited to only one full operating cycle for Braidwood 1
ending in spring 1997 and for the operating cycle ending in late 1997
for Byron 1.
Additionally, the inspection and reporting requirements added to
the Byron 1 and Braidwood 1 TSs by the prior amendments cited above,
would also be continued for one more operating cycle for both units.
The maximum permissible value of the iodine-131 concentration in the
primary coolant in both the Byron 1 and Braidwood 1 TSs remains
unchanged at 0.35 microcuries per gram of coolant. Finally, the Bases
sections in the Byron 1 and Braidwood 1 TSs are proposed to be revised
to introduce the terminology associated with the Locked-Tube SG tube
model and that of the Free-Span model.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
This amendment request proposes to renew the SG tube plugging/
repair criteria previously approved by the NRC in Amendments 69 and
77 to Braidwood and Byron Technical Specifications, respectively.
The previously evaluated applicable accidents are steam
generator tube burst and Main Steam Line Break (MSLB). The
postulated MSLB outside of containment but upstream of the Main
Steam Isolation Valve (MSIV) represents the most limiting
radiological condition relative to the IPC. The potential impact on
public health and safety as a result of renewing the SG tube interim
plugging criteria contained in the current Braidwood and Byron
Technical Specifications is very low as discussed below. Tube burst
due to predominantly axially oriented ODSCC at the TSP intersections
is precluded during normal operating plant conditions since the tube
support plates are adjacent to the degraded regions of the tube in
the tube-to-tube support plate crevices.
During accident conditions, i.e., MSLB, the tubes and TSP may
move relative to each other. This can expose the crack length
portion to free-span conditions. Testing has shown that the burst
pressure correlates to the crack length that is exposed to the free-
span, regardless of the length that is still contained within the
TSP bounds.
Therefore, a more appropriate methodology has been established
for addressing leakage and burst considerations. This methodology is
based on limiting potential TSP displacements (Locked-Tube Model
Intersections) during postulated MSLB events, thus reducing the
free-span exposed crack length to minimal levels. The tube expansion
process employed in conjunction with this tube plugging criteria is
designed to provide postulated TSP displacements that result in
negligible tube burst probabilities due to the minimal free-span
exposed crack lengths. The tube expansions were performed during the
first outage that the 3.0 volt IPC was applied (Braidwood refuel
outage A1R05 -Fall 1995, and Byron midcycle outage B1P02 - Fall
1995). These expansions will be inspected in accordance with an eddy
current inspection probe that is sensitive to axial and
circumferential indications. This program will ensure the integrity
of the expansions for the additional cycle of operation. It has been
demonstrated that axial indications in the expansion region will not
result in a reduction of the load carrying capability of the
expanded tubes.
Thermal hydraulic modeling was used to determine TSP loading
during MSLB conditions. A safety factor was conservatively applied
to these loads to envelope the collective uncertainties in the
analyses. Various operating conditions were evaluated and the most
limiting operating condition was used in the analyses. Additional
models were used to verify the thermal hydraulic results.
Assessment of the tube burst probability for the Locked-Tube
Model Intersections was based on a conservative assumption that all
hot-leg TSP intersections (32,046) contained through wall cracks
equal to the postulated TSP displacement and that the crack lengths
were located within the boundaries of the TSP. Alternatively, it was
assumed that all hot-leg TSP intersections contained through wall
cracks with lengths equal to the thickness of the TSP. The
postulated TSP motion was conservatively assumed to be uniform and
equal to the maximum displacement calculated.
The total burst probability for all 32,046 through wall
indications, given a uniform MSLB TSP displacement of 0.31 inches,
was calculated to be 1x10-5. This is a factor of 1000 less than
the GL 95-05 burst probability limit of 1x10-2. Therefore, the
functional design criteria for tube expansion was to limit the TSP
motion to 0.31'' or less. However, the design goal for tube
expansion limits the TSP MSLB motion to less than 0.1''. This design
goal results in a total tube burst probability of 1x10-10 for
all 32,046 postulated through wall indications. Additional tubes
were expanded to provide redundancy for the required expansions.
The structural limit for the Locked-Tube Model Intersection SG
tube repair criteria was based on axial tensile loading requirements
to preclude axial tensile severing of the tube. Axially oriented
ODSCC does not significantly impact the axial tensile loading of the
tube. Based on the current voltage distributions and growth rates,
Monte Carlo projections were performed for Braidwood Unit 1 and
Byron Unit 1 for the additional cycle of operation that this
proposed amendment is requesting. The End of Cycle (EOC) voltage
projections for Braidwood Unit 1 Cycle 7 predict that the maximum
voltage to be seen will be less than 10.5 volts. The number of
indications predicted greater than ten volts at the end of Cycle 7
for Braidwood Unit 1 is 0.3. The EOC voltage projections for Byron
Unit 1 Cycle 9 predict that the maximum voltage to be seen will be
less than 13.5 volts. The number of indications predicted greater
than ten volts at the end of Cycle 9 for Byron Unit 1 is 4.59.
Using a tensile rupture probability for a ten volt indication of
3x10-6, the probability of tensile rupture from the predicted
0.3 indications at Braidwood is 1-(1-3x10-6)0.3 =
9.0x10-7. The probability of tensile rupture from the predicted
4.59 indications at Byron is 1-(1-3x10-6)4.59 =
1.38x10-5. Both of these probabilities result in a negligible
contribution to the total burst probability when compared to the
1x10-2 GL 95-05 limit.
Cellular corrosion is a more limiting mode of degradation at the
TSPs with respect to affecting the tube structural limit. Tensile
tests that measure the force required to sever a tube with cellular
corrosion and uncorroded cross sectional areas are used to establish
the lower bound structural limit. Based upon these tests, a lower
bound 95% confidence level structural voltage limit of 37 volts was
established for cellular corrosion. This limit meets the Regulatory
Guide (RG) 1.121, ``Basis for Plugging Steam Generator Tubes,''
structural requirements based upon the normal operating pressure
differential with a safety factor of 3.0 applied. Due to the limited
database supporting this value, the
[[Page 6571]]
structural limit was conservatively reduced to 20 volts. Accounting
for voltage growth and Non-Destructive Examination (NDE)
uncertainty, the full IPC upper limit exceeds ten volts. However,
for added conservatism a single voltage repair limit of 3.0 volts
for the Locked-Tube Model Intersection indications is specified in
the current plugging/repair criteria. All indications at the Locked
Tube Model Intersections with bobbin coil probe voltages greater
than 3.0 volts will be plugged or repaired.
The free-span tube burst probability must be calculated for the
indications at the Free-Span Model Intersections. The total burst
probability must be within the requirements of GL 95-05. The free-
span structural voltage limit is calculated using correlations from
the database described in GL 95-05, with the inclusion of the recent
Byron, Braidwood, and South Texas tube pull results. The structural
limit for the Free-Span Model Intersections is 4.745 volts. The
lower voltage repair limit for the indications at the Free-Span
Model Intersections continues to be 1.0 volt. The upper voltage
repair limit for the indications at the Free-Span Model
Intersections will be calculated in accordance with GL 95-05.
Since IPC will not be applied to indications at the Flow
Distribution Baffle (FDB), no leakage or burst analyses are required
for these indications.
Per GL 95-05, MSLB leak rate and tube burst probability analyses
are required to be performed prior to returning the unit to power.
The results of these analyses are to be included in a report to the
NRC within 90 days of restart. If allowable limits on leak rates and
burst probability are exceeded, the results are to be reported to
the NRC and a safety assessment of the significance of the results
is to be performed prior to returning the SGs to service.
A site specific calculation has determined the site allowable
leakage limit for Braidwood and Byron. These limits use the
recommended Dose Equivalent Iodine-131 transient spiking values
consistent with NUREG-0800, ``Standard Review Plan'' and ensure site
boundary doses are within a small fraction of the 10 CFR 100
requirements.
The projected leakage rate calculation methodology described in
WCAP-14046, ``Braidwood Unit 1 Technical Support for Cycle 5 Steam
Generator Interim Plugging Criteria,'' and WCAP-14277, ``SLB Leak
Rate and Tube Burst Probability Analysis Methods for ODSCC at TSP
Intersections,'' will be used to calculate the EOC leakage. This
method includes a Probability of Detection (POD) value of 0.6 for
all voltage amplitude ranges and uses the accepted leak rate versus
bobbin voltage correlation methodology (full Monte Carlo) for
calculating the leak rate, as described in GL 95-05. The database
used for the leak and burst correlations is consistent with that
described in GL 95-05 with the inclusion of the Byron Unit 1,
Braidwood Unit 1, and South Texas tube pull results. The EOC voltage
distribution is developed from the POD adjusted beginning-of-cycle
(BOC) voltage distributions and uses Monte Carlo techniques to
account for variances in growth and NDE uncertainty.
The Electric Power Research Institute (EPRI) leak rate
correlation has been used. This correlation is based on free-span
indications that have burst pressures above the MSLB pressure
differential. There is a low but finite probability that indications
may burst at a pressure less than MSLB pressure. With limited TSP
motion for the Locked-Tube Model Intersections, the tube is
constrained by the TSP and tube burst is precluded. However, the
flanks of the crack may open up to contact the Inside Diameter (ID)
of the TSP hole and result in a primary-to-secondary leak rate
potentially exceeding that obtained from the EPRI correlation. This
phenomenon is known as an Indication Restricted from Burst (IRB)
condition.
ComEd has performed laboratory testing to determine the bounding
leak rate obtainable in an IRB condition (6.0 gallons per minute).
The bounding leak rate value was then applied to a leak rate
calculation methodology that accounts for the MSLB leak rate
contribution from IRB indications to the total leak rate calculated
as described above. Results indicate that the IRB contribution to
the total leak rate value is negligible. However, ComEd will
conservatively add a leakage contribution due to IRBs in addition to
the leakage calculated in accordance with GL 95-05. When this is
done, the dose at the site boundary resulting from the predicted
leakage will be a small fraction (less than 10%) of the 10 CFR 100
limits.
Modification of the Braidwood and Byron TS to clarify
application of the proposed tube plugging/repair criteria is purely
administrative and will not have any effect on the probability or
consequences of an accident previously evaluated.
Operating experience over the last cycle with this plugging
criteria applied has not revealed any unpredicted or unusual
effects.
For these reasons, renewal of the current Braidwood and Byron
tube plugging criteria does not adversely affect SG tube integrity
and results in acceptable dose consequences. By effectively
eliminating tube burst at the Locked-Tube Model TSP intersections,
the likelihood of a tube rupture is substantially reduced and the
probability of occurrence of an accident previously evaluated is
reduced.
This conclusion is not affected by foreign or domestic plant SG
experiences (NRC Information Notice 96-09 and its supplement). As
the following evaluation shows, these experiences are not relevant
to Braidwood or Byron.
A foreign unit detected eddy current signal distortions in one
area of the top TSP during a 1995 inspection. The steam generators
had been chemically cleaned in 1992. Visual inspection showed that a
small section of the top TSP had broken free and was resting next to
the steam generator tube bundle wrapper. The support plate showed
indications of metal loss.
The chemical cleaning process used by the foreign unit was
developed by the utility and differs significantly from the modified
EPRI/SGOG process performed at Byron Unit 1 in 1994. The foreign
chemical cleaning process, coupled with the specific application of
the process, resulted in TSP corrosion of up to 250 mils compared to
a maximum of 2.16 mils (11 mils maximum allowed) measured at Byron.
During the Byron eddy current inspection performed after the
chemical cleaning, no distortion of the tube support plate signals
was reported. Therefore, these differences in cleaning processes
imply that this foreign experience is irrelevant to the effects of
the chemical cleaning process on the TSPs at Byron. Chemical
cleaning of the SGs has not occurred at Braidwood.
A number of units have experienced TSP cracking associated with
severe tube denting due to TSP corrosion at the tube-to-TSP crevice.
WCAP-14273, Section 12.4, shows that a diametral reduction of a SG
tube of 0.065 inches is required to develop stress levels above
yield in the TSP ligaments at dented intersections. The bobbin
voltage range associated with a one mil radial dent is twenty to
twenty-five volts.
Although Braidwood Unit 1 and Byron Unit 1 have not seen
corrosion induced denting, a 0.610 inch diameter bobbin coil probe
will be used as a go/no-go gauge to assess dents at the Locked-Tube
Model Intersections, if they occur in the future. If a tube has a
dent at a Locked-Tube Model TSP intersection that fails to pass the
go/no-go test probe, IPC will not be applied to that intersection.
In addition, if the dent is determined to be corrosion induced, the
Free-Span Model repair criteria will be applied to the intersections
adjacent to the dented intersection. IPC repair limits will not be
applied to tubes with dents greater than 5.0 volts since dent
signals of this magnitude could mask a 1.0 volt ODSCC signal. Tube
intersections with corrosion induced dents greater than 5.0 volts
and the intersections adjacent to such an intersection were not
selected for tube expansion to preclude adverse effects of the
failure of such a tube on limiting TSP displacement. If corrosion
induced denting, either greater than 5.0 volts or such that the tube
is unable to pass a 0.610 inch diameter bobbin coil probe, are
detected at an intersection adjacent to an expanded intersection,
the dented intersection will be inspected by an EPRI developed
technique to determine if the TSP is cracked. If a crack-like
indication is identified in a TSP, a plus point inspection will be
conducted per the EPRI TSP program. If the plus point inspection
verifies the existence of a crack-like indication, the effect of
that indication on TSP displacement will be evaluated. If this
evaluation shows that TSP displacement would be greater than 0.1
inches during a MSLB event, the effected area will either be
mechanically corrected or the Free-Span Model criteria will be
applied to the affected area. Based on the information presented
above, the SG tube denting experience at other plants is not
relevant to Braidwood or Byron.
A foreign utility's SGs have experienced cracking at the top
TSP. The cause of the cracking appears to be the configuration of
the single anti-rotation device, connected between the SG shell and
wrapper, and the wrapper internals. The single anti-rotation device
carries the full load associated with the wrapper to shell motion.
This rotational load is believed to be transferred to the TSP via
the wrapper internals. The Byron/Braidwood Unit 1 SG design (D-4)
uses three anti-rotation devices to spread the rotational load. The
D-4 wrapper internals are configured such that this load is not
directly transmitted to the TSP.
[[Page 6572]]
No top TSP cracking has been detected at Braidwood Unit 1 or
Byron Unit 1 and very few (<1%) of="" the="" odscc="" indications="" in="" the="" sg="" tubes="" at="" braidwood="" and="" byron,="" to="" date,="" have="" been="" at="" the="" top="" tsp="" elevation.="" nevertheless,="" an="" analysis="" was="" performed="" to="" assess="" the="" impact="" of="" cracking="" of="" the="" top="" tsp.="" the="" results="" show="" an="" increase="" in="" the="" deflection="" of="" the="" top="" tsp="" for="" a="" very="" limited="" number="" of="" tubes="" to="" greater="" than="" the="" 0.10''="" limit="" used="" in="" the="" 3.0="" volt="" ipc="" analysis.="" the="" deflections="" of="" the="" lower="" support="" plates="" also="" increased,="" but="" remain="" within="" the="" 0.10''="" limit.="" thus,="" a="" large="" majority="" of="" the="" locked-tube="" model="" indications="" continue="" to="" be="" bounded="" by="" the="" existing="" analysis="" even="" with="" a="" cracked="" top="" tsp.="" the="" locked-tube="" model="" repair="" criteria="" will="" not="" be="" applied="" to="" any="" sg="" tube="" odscc="" indication="" where="" the="" tsp="" has="" been="" shown="" to="" be="" displaced="" by="" more="" than="" 0.1="" inches="" during="" accident="" conditions.="" in="" response="" to="" these="" experiences="" at="" foreign="" and="" domestic="" utilities,="" comed="" developed="" an="" inspection="" plan="" for="" the="" sg="" internals="" to="" identify="" if="" indications="" detrimental="" to="" the="" load="" path="" components="" existed.="" this="" inspection="" plan="" was="" carried="" out="" at="" braidwood="" during="" refueling="" outage="" a1r05="" (fall="" 1995)="" and="" at="" byron="" during="" the="" midcycle="" outage="" b1p02="" (fall="" 1995)="" and="" refuel="" outage="" b1r07="" (spring="" 1996).="" these="" inspections="" revealed="" no="" degradation="" of="" the="" sg="" load="" path="" components="" necessary="" to="" support="" implementation="" of="" the="" 3.0="" volt="" ipc.="" inspections="" will="" be="" performed="" during="" the="" upcoming="" refuel="" outages="" at="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" to="" further="" ensure="" the="" integrity="" of="" the="" sg="" load="" path="" components="" necessary="" to="" support="" implementation="" of="" the="" 3.0="" volt="" ipc.="" a="" domestic="" utility="" reported="" several="" distorted="" tsp="" signals="" over="" the="" past="" three="" refueling="" outages'="" sg="" tube="" inspections.="" it="" was="" determined="" that="" these="" signals="" were="" associated="" with="" the="" tsp="" geometry="" in="" an="" area="" where="" an="" access="" cover="" is="" welded="" to="" the="" tsp.="" these="" signal="" distortions="" are="" not="" attributed="" to="" tsp="" cracking="" or="" degradation.="" since="" the="" distorted="" signals="" were="" due="" to="" tsp="" geometry="" which="" did="" not="" indicate="" or="" result="" in="" a="" defect="" of="" the="" tsp,="" there="" is="" no="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" due="" to="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" steam="" generator="" tsp="" geometries="" which="" may="" result="" in="" distorted="" eddy="" current="" signals.="" one="" foreign="" unit="" observed="" a="" dislocation="" of="" the="" tube="" bundle="" wrapper="" when="" they="" were="" unable="" to="" pass="" sludge="" lancing="" equipment="" through="" a="" hand="" hole="" in="" the="" wrapper.="" the="" dislocation="" appears="" to="" be="" a="" result="" of="" improper="" attachment="" of="" the="" wrapper="" to="" the="" support="" structure.="" sg="" sludge="" lance="" operations="" have="" been="" successfully="" performed="" at="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" which="" indicates="" that="" no="" problem="" with="" the="" wrapper="" attachment="" exists.="" the="" foreign="" unit's="" wrapper="" support="" design="" is="" significantly="" different="" than="" that="" used="" on="" braidwood="" unit="" 1="" and="" byron="" unit="" 1.="" therefore,="" a="" similar="" wrapper="" dislocation="" will="" not="" occur="" and="" the="" foreign="" experience="" is="" not="" applicable="" to="" braidwood="" or="" byron.="" an="" inspection="" was="" conducted="" during="" the="" last="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" refueling="" outages="" which="" verified="" this="" conclusion.="" comed="" will="" continue="" to="" apply="" a="" maximum="" primary-to-secondary="" leakage="" limit="" of="" 150="" gallons="" per="" day="" (gpd)="" through="" any="" one="" sg="" at="" braidwood="" and="" byron="" to="" help="" preclude="" the="" potential="" for="" excessive="" leakage="" during="" all="" plant="" conditions.="" the="" rg="" 1.121="" criterion="" for="" establishing="" operational="" leakage="" limits="" that="" require="" plant="" shutdown="" are="" based="" on="" detecting="" a="" free-span="" crack="" prior="" to="" it="" resulting="" in="" primary-to-secondary="" operational="" leakage="" which="" could="" potentially="" develop="" into="" a="" tube="" rupture="" during="" faulted="" plant="" conditions.="" the="" 150="" gpd="" limit="" provides="" for="" leakage="" detection="" and="" plant="" shutdown="" in="" the="" event="" of="" an="" unexpected="" single="" crack="" leak="" associated="" with="" the="" longest="" permissible="" free-span="" crack="" length.="" therefore,="" the="" proposed="" amendment="" does="" not="" result="" in="" any="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" within="" the="" braidwood="" and="" byron="" updated="" final="" safety="" analysis="" report="" (ufsar).="" 2.="" the="" proposed="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" this="" amendment="" request="" proposes="" to="" renew="" the="" sg="" tube="" plugging/="" repair="" criteria="" previously="" approved="" by="" the="" nrc="" in="" amendments="" 69="" and="" 77="" to="" braidwood="" and="" byron="" technical="" specifications,="" respectively.="" renewal="" of="" the="" proposed="" steam="" generator="" tube="" plugging="" criteria="" with="" tube="" expansion="" does="" not="" introduce="" any="" significant="" changes="" to="" the="" plant="" design="" basis.="" use="" of="" the="" criteria="" does="" not="" provide="" a="" mechanism="" which="" could="" result="" in="" an="" accident="" outside="" of="" the="" region="" of="" the="" tube="" support="" plate="" elevations="" as="" odscc="" does="" not="" extend="" beyond="" the="" thickness="" of="" the="" tube="" support="" plates="" and="" ipc="" is="" not="" allowed="" to="" be="" applied="" to="" indications="" that="" extend="" beyond="" the="" thickness="" of="" the="" tube="" support="" plate.="" neither="" a="" single="" nor="" multiple="" tube="" rupture="" event="" would="" be="" expected="" in="" a="" sg="" in="" which="" the="" plugging="" criteria="" has="" been="" applied.="" the="" tube="" burst="" assessment="" involves="" a="" monte="" carlo="" simulation="" of="" the="" site="" specific="" voltage="" distribution="" to="" generate="" a="" total="" burst="" probability="" that="" includes="" the="" summation="" of="" the="" probabilities="" of="" one="" tube="" bursting,="" two="" tubes="" bursting,="" etc.="" for="" the="" locked-tube="" model="" tsp="" intersections,="" the="" maximum="" total="" probability="" of="" burst,="" by="" design,="" is="" estimated="" to="" be="">1%)>-10 with all tube expansions
functional. The burst probability for the Free-Span Model TSP
intersections will be dependent on the number and size of
indications at these applicable intersections. The total burst
probability will be within the limit specified in GL 95-05.
Accounting for the unlikely event of a failure of the expanded
tubes, a sufficient number of redundant expansions exist to ensure
that the burst probability remains below 1x10-5. This includes
the conservative assumption that all 32,046 hot-leg TSP
intersections contain through wall indications. This level of burst
probability is considered to be negligible when compared to the GL
95-05 limit of 1x10-2.
In addressing the combined effects of a Loss Of Coolant Accident
(LOCA) during a Safe Shutdown Earthquake (SSE) on the SG as required
by General Design Criteria (GDC) 2, it has been determined that tube
collapse may occur in the steam generators at some plants. The tube
support plates may become deformed as a result of lateral loads at
the wedge supports located at the periphery of the plate due to the
combined effects of the LOCA rarefaction wave and SSE loadings. The
resulting pressure differential on the deformed tubes may cause some
of the tubes to collapse. There are two issues associated with SG
tube collapse. First, the collapse of SG tubing reduces the Reactor
Coolant System (RCS) flow area through the tubes. The reduction in
flow area increases the resistance to flow of steam from the core
during a LOCA which, in turn, may potentially increase the Peak Clad
Temperature (PCT). Second, there is a potential that partial through
wall cracks in the SG tubes could progress to through wall cracks
during tube deformation or collapse. The tubes subject to collapse
have been identified via a plant specific analysis and are excluded
from application of any voltage-based criteria. This analysis is
included in revision 3 to WCAP-14046 which was submitted to the NRC
June 19, 1995.
Modification of the Braidwood and Byron Technical Specifications
to clarify application of the proposed tube plugging/repair criteria
is purely administrative and will not create the possibility of a
new or different kind of accident from any accident previously
evaluated.
Operating experience over the last cycle with this plugging
criteria applied has not revealed any unpredicted or unusual
effects.
SG tube integrity will continue to be maintained following
renewal of the 3.0 volt IPC voltage repair limit through inservice
inspection, tube repair and primary-to-secondary leakage monitoring.
By effectively eliminating tube burst at the Locked-Tube Model TSP
Intersections, the potential for multiple tube ruptures is
essentially eliminated.
ComEd has evaluated industry experiences with TSP degradation,
eddy current signal distortions, and component misalignment. Eddy
current signal distortions due to TSP geometry are not indicative of
TSP degradation and do not result in any kind of new or different
accident.
The component misalignment experienced by one unit is not
applicable to Braidwood Unit 1 or Byron Unit 1 and, thus, will not
result in any kind of new or different accident. Specific
limitations, as discussed in response to Question 1, will be applied
to indications at the Locked-Tube Model Intersections which contain
dents. These limitations ensure that the integrity of the SG tubes
is maintained consistent with the current analyses should tube
denting or TSP cracking occur.
Therefore, renewal of the current tube plugging/repair criteria
at Braidwood Unit 1 and Byron Unit 1 will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. The proposed change does not involve a significant reduction
in a margin of safety.
The use of the voltage-based, bobbin coil, tube support plate
plugging criteria with tube expansion at Braidwood Unit 1 and Byron
Unit 1 is demonstrated to maintain SG tube integrity commensurate
with the criteria of RG 1.121. RG 1.121 describes a method
[[Page 6573]]
acceptable to the NRC staff for meeting GDC 14, 15, 31, and 32 by
reducing the probability or the consequences of steam generator tube
rupture.
Reducing the probability or the consequences of steam generator
tube rupture is accomplished by determining an eddy current
inspection voltage value which represents a limit for leaving an
axial, crack-like indication at an in service SG tube TSP
intersection. Tubes with ODSCC voltage indications beyond this
limiting value must be removed from service by plugging or repaired
by sleeving. Implementation of a 3.0 volt IPC voltage repair limit
for the Locked-Tube Model Intersections has been evaluated and shown
not to present a credible potential for a steam generator tube
rupture event during normal or faulted plant conditions, even with
worst case assumptions. The total tube burst probability will
include a contribution from the indications at the Locked-Tube Model
Intersections and from indications at the Free-Span Model
Intersections. The projected EOC voltage distribution of crack-like
indications at the TSP elevations will be confirmed to result in
acceptable primary-to-secondary leakage during all plant conditions
such that radiological consequences are not adversely impacted.
Addressing RG 1.83 considerations, implementation of the
increased Locked-Tube Model Intersection bobbin coil voltage-based
repair criteria is supplemented by enhanced eddy current inspection
guidelines to provide consistency in voltage normalization and a
100% eddy current inspection sample size at the affected TSP
elevations.
For the leak and burst assessments, the population of
indications in the EOC voltage distribution is dependent on the POD
function. The purpose of the POD function is to account for new
indications that may develop over the cycle, and to account for
indications not identified by the data analyst. In implementing this
proposed IPC renewal, ComEd will continue to use the conservative GL
95-05 POD value of 0.6 for all voltage amplitude ranges.
Modification of the Braidwood and Byron Technical Specifications
to clarify application of the proposed tube plugging/repair criteria
is purely administrative and will not reduce any safety margins.
Operating experience over the last cycle with this plugging
criteria applied has not revealed any unpredicted or unusual
effects.
Implementation of the TSP elevation repair limits will decrease
the number of tubes which must be repaired. Installation of steam
generator tube plugs or sleeves reduces the RCS flow margin. Thus,
implementation of the IPC will maintain the margin of flow that
would otherwise be reduced in the event of increased tube plugging
or sleeving.
As discussed previously, ComEd has evaluated industry
experiences with TSP degradation, eddy current signal distortions,
and component misalignment. Eddy current signal distortions at tube
support plates will be evaluated to attempt to determine the cause
of the distortion. A signal distortion alone will not result in
reduction in the margin of safety. The foreign unit that experienced
the component misalignment was of a significantly different design
than the Braidwood Unit 1 and Byron Unit 1 steam generators.
Analysis of the design differences shows that component misalignment
of that type is not applicable to Braidwood Unit 1 or Byron Unit 1
and, thus, will not result in a reduction in the margin of safety.
An inspection was conducted during the last Braidwood Unit 1 and
Byron Unit 1 refueling outages which verified this conclusion.
Specific limitations, as discussed previously, will be applied
to indications at the Locked-Tube Model Intersections which contain
dents. These limitations conservatively treat indications as free-
span to ensure that the integrity of the SG tubes is maintained
consistent with current analyses should tube denting or TSP cracking
occur. Application of the 3.0 volt Locked-Tube Model Intersection
IPC and the 1.0 volt Free-Span Model Intersection IPC at Braidwood
Unit 1 and Byron Unit 1, with the limitations specified, will not
result in a reduction in a margin of safety.
Thus, the implementation of this amendment does not result in a
significant reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
requested amendments involve no significant hazards consideration.
Local Public Document Room location: For Byron, the Byron Public
Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010;
for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street,
Wilmington, Illinois 60481.
Attorney for licensee: Michael I. Miller, Esquire; Sidley and
Austin, One First National Plaza, Chicago, Illinois 60603.
NRC Project Director: Robert A. Capra
Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden
Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station,
Units 1 and 2, Rock Island County, Illinois
Date of application for amendment request: January 6, 1997
Description of amendment request: The proposed amendment would
clarify and maintain consistency between the operability requirements
for protective instrumentation and associated automatic bypass
features.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1) Involve a significant increase in the probability or consequences of
an accident previously evaluated because of the following:
The proposed changes are administrative in nature and do not
affect the probability or consequences of any previously evaluated
accidents for Dresden or Quad Cities Stations. The proposed
amendment is consistent with the current safety analyses and
represents sufficient requirements for the continued assurance and
reliability of the RPS and Rod Block Instrumentation equipment,
which is assumed to operate in the safety analysis, or provides
continued assurance that specified parameters associated with RPS
and Rod Block Instrumentation remain within their acceptance limits.
Therefore, these changes will not affect the probability or
consequences of a previously evaluated accident.
The RPS and Rod Block Instrumentation related to this proposed
amendment is not assumed in any safety analysis to initiate any
accident sequence for Dresden or Quad Cities Stations; therefore,
the probability of any accident previously evaluated is not affected
by the proposed amendment.
2) Create the possibility of a new or different kind of accident
from any accident previously evaluated because:
The proposed changes are administrative in nature and serve to
maintain consistent and clear requirements for operability as
specified in the Technical Specifications for the Limiting
Conditions for Operation and Surveillance Requirements for the RPS
and Rod Block Instrumentation. No new modes of operation or changes
to any plant equipment are proposed by the proposed amendment
request. The associated systems related to this proposed amendment
are not assumed in any safety analysis to initiate any accident
sequence for Dresden or Quad Cities. The proposed changes maintain
the present level of operability; and therefore, the proposed
changes do not create the possibility of a new or different kind of
accident than any previously evaluated.
3) Involve a significant reduction in the margin of safety
because:
The proposed changes are administrative in nature and do not
affect existing plant safety margins or the reliability of the
equipment assumed to operate in the safety analysis. The proposed
changes have been evaluated and found to be acceptable for use at
Dresden and at Quad Cities based on RPS and Rod Block
Instrumentation system design, safety analysis requirements and
operational performance. Since the proposed changes are
administrative in nature and maintain necessary levels of the RPS
and Rod Block reliability, the proposed changes do not involve a
reduction in the margin of safety.
The proposed amendment for Dresden and Quad Cities Stations will
not reduce the availability of the RPS and Rod Block Instrumentation
System which is required to mitigate accident conditions; therefore,
the proposed changes do not involve a reduction in the margin of
safety.
The NRC staff has reviewed the licensee's analysis and, based on
this
[[Page 6574]]
review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: for Dresden, Morris Area
Public Library District, 604 Liberty Street, Morris, Illinois 60450;
for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon,
Illinois 61021
Attorney for licensee: Michael I. Miller, Esquire; Sidley and
Austin, One First National Plaza, Chicago, Illinois 60603
NRC Project Director: Robert A. Capra
Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment request: October 22, 1996
Description of amendment request: The proposed amendments would
allow continued plant operation at elevated Containment Lower
Compartment temperatures between 125 deg. and 135 deg. F for a period
not to exceed 72 cumulative hours.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. Does the proposed amendment involve a significant increase in
the probability or consequences of any accident previously evaluated
in the UFSAR [Updated Final Safety Analysis Report]?
The increase in maximum Containment Lower Compartment
temperature will not change the operation of any equipment which is
important to safety. All components and instruments will continue to
perform as designed in the higher temperature environment for the
period that the revised Technical Specification allows. This
temperature increase will not impact the ability of any component or
instrument to perform its function in the event of an accident.
Therefore, the probability of an accident is not impacted. The
increased temperature will cause a decrease in the air mass in lower
containment. This change has been evaluated for impact on
containment temperature and pressure in accident conditions. The air
mass change is conservative for peak containment pressure since the
air mass is decreased. Maximum containment temperatures during a
postulated accident are slightly increased as a result of higher
initial Containment Lower Compartment temperature. The increase in
peak temperature remains within the allowable values and thus does
not increase the probability or consequence of an accident. The
minimum containment pressure as a result of steam condensation in
containment is lowered as a result of the decreased air mass in
containment. Due to the conservative assumptions made in modeling
containment for minimum pressure response, this change has no impact
on the accident analysis.
Based on the analysis of the bounding accidents that may be
impacted by increased Containment Lower Compartment temperature and
the review of the effect of the increased temperature on components
in lower containment, it is determined that the probability and
consequence of any analyzed accident is unchanged as a result of
this change.
2. Does the proposed amendment create the possibility of a new
or different kind of accident not previously evaluated?
The revised maximum Containment Lower Compartment temperature
will not change any systems or operations procedures except to
procedurally respond should Containment Lower Compartment
temperature remain elevated for a period near the revised limiting
period. The response of the systems and components are unaffected by
this change. All instruments are qualified for the revised service
conditions and will perform in the same manner as before. Normal
operation and transient response will remain unchanged. Review of
previously analyzed accidents show that no new transients are
created as a result of this change. Based on this review there are
no new or different accidents made possible by this change.
3. Does the proposed amendment involve a significant reduction
in a margin of safety?
The amendment could potentially affect the containment system.
The operation and analysis of the reactor coolant system and fuel
are unaffected by this change. The maximum containment temperature
is slightly increased while the maximum containment pressure is
decreased. The minimum containment pressure could be slightly
decreased and minimum containment temperature is unaffected. All
these parameters have been reviewed and determined to be within
assumptions made in these analyses. The accident transient analyses
are unaffected beyond these small changes and remains acceptable in
all cases. Therefore, the margin of safety is unaffected by this
amendment.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: J. Murrey Atkins Library,
University of North Carolina at Charlotte, 9201 University City
Boulevard, North Carolina 28223-0001
Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422
South Church Street, Charlotte, North Carolina 28242
NRC Project Director: Herbert N. Berkow
Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment request: January 6, 1997
Description of amendment request: The proposed amendments would
allow a one-time revision to Technical Specifications 3.6.1.1, 3.6.1.2,
3.6.1.8, and 3.6.1.9 to allow operation of the Containment Purge
Ventilation System (VP) during Modes 3 and 4 following the steam
generator (SG) replacement outage. This one-time revision would be
necessary due to respiratory hazardous gases released during heatup
after the replacement of the SGs. The VP system would be used to remove
the hazardous gases.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. The activity does not involve a significant increase in the
probability or consequences of an accident previously evaluated.
The VP [Containment Purge Ventilation] System has no interfaces
with any primary system, secondary system, or power transmission
system. It has no interfaces with any reservoir of radioactive gases
or liquids. None of the systems listed above are modified by the
activity. In summary, no ``accident initiator'' is affected with the
proposed operation of the VP System in Modes 3 and 4. For this
reason, the activity does not involve an increase in the probability
of an accident previously evaluated.
Analyses have been performed to determine upper bounds to the
source term, the offsite doses, and the Control Room dose. The
results of that analyses are reported above. Both the source term
and the doses were found to be significantly lower than the results
of the corresponding design basis analyses. In addition, it has been
determined that with no credit taken for any heat transfer from the
fuel and cladding to the moderator channels, that sufficient time
would exist for the operators to initiate recovery of flow from the
ECCS [Emergency Core Cooling System] to the reactor core. The flow
required from the ECCS to maintain the core in a coolable geometry
was found to be well within the capacity of any one ECCS pump.
Furthermore, it was determined that convective heat transfer to
steam would be sufficient to prevent release of significant source
term or a significant degree of fuel damage.
For the above reasons, it is determined that operation of the VP
System in Mode 3 or 4 immediately following the steam generator
replacement outage does not involve a significant increase in either
the probability or the consequences of an accident previously
evaluated.
2. The activity does not create the possibility of a new or
different type of
[[Page 6575]]
accident from any accident previously evaluated.
As discussed above, no ``accident initiators'' are affected by
the proposed activity. Operation of the VP System proposed for Modes
3 and 4 will be the same as that routinely carried in other modes of
operation. For these reasons, the activity will not create the
possibility of a new or different type of accident from any
previously evaluated.
3. The activity does not involve a significant reduction in the
margin of safety.
Margin of safety is associated with confidence in the ability of
the fission product barriers (the fuel and fuel cladding, the
Reactor Coolant System pressure boundary, and the containment) to
limit the level of radiation doses to the public. The proposed
operation of the VP System will occur at the end of an extended
outage. The level of decay heat and activity in the reactor is very
low compared to the level of decay heat and activity associated with
full power operations. For this reason, the likelihood of damage to
the fuel following a DBLOCA [design basis loss-of-coolant accident]
occurring during the proposed purging is reduced, as determined
above. Both offsite doses and doses to the Control Room were found
to be small compared to the limits of 10 CFR [Part] 100 and GDC
[General Design Criterion] 19. For these reasons, the activity does
not involve a significant reduction in the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: J. Murrey Atkins Library,
University of North Carolina at Charlotte, 9201 University City
Boulevard, North Carolina 28223-0001
Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422
South Church Street, Charlotte, North Carolina 28242
NRC Project Director: Herbert N. Berkow
Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear
Station, Units 1 and 2, Mecklenburg County, North Carolina
Date of amendment request: January 13, 1997
Description of amendment request: The proposed amendments would
implement the performance-based containment leak rate testing
requirements of 10 CFR Part 50, Appendix J, Option B, for Type A
testing.
Compliance with 10 CFR Part 50, Appendix J, provides assurance that
the primary containment, including those systems and components that
penetrate the primary containment, do not exceed the allowable leakage
rate values specified in the Technical Specifications and Bases. The
allowable leakage rate is determined so that the leakage assumed in the
safety analyses is not exceeded.
On February 4, 1992, the NRC published a notice in the Federal
Register (57 FR 4166) discussing a planned initiative to begin
eliminating requirements marginal to safety that impose a significant
regulatory burden. Appendix J to 10 CFR Part 50, ``Primary Containment
Leakage Testing for Water-Cooled Power Reactors,'' was considered for
this initiative and the staff undertook a study of possible changes to
this regulation. The study examined the previous performance history of
domestic containments and examined the effect on risk of a revision to
the requirements of Appendix J. The results of this study are reported
in NUREG-1493, ``Performance-Based Leak-Test Program.''
Based on the results of this study, the staff developed a
performance based approach to containment leakage rate testing. On
September 12, 1995, the NRC approved issuance of this revision to 10
CFR Part 50, Appendix J, which was subsequently published in the
Federal Register on September 26, 1995, and became effective on October
26, 1995. The revision added Option B ``Performance-Based
Requirements'' to Appendix J to allow licensees to voluntarily replace
the prescriptive testing requirements of Appendix J with testing
requirements based on both overall and individual component leakage
rate performance.
Regulatory Guide 1.163, ``Performance-Based Containment Leak Test
Program,'' was developed as a method acceptable to the staff for
implementing Option B. Accordingly, the licensee has submitted, in its
application dated January 13, 1997, proposed changes to the TS to
implement 10 CFR Part 50, Appendix J, Option B, by referring to
Regulatory Guide 1.163, ``Performance-Based Containment Leakage-Test
Program.''
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. The proposed change will not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
Containment leak rate testing is not an initiator of any
accident; the proposed change does not affect reactor operations or
accident analysis, and has no significant radiological consequences.
... Therefore, this proposed change will not involve an increase in
the probability or consequences of any previously-evaluated
accident.
2. The proposed change will not create the possibility of any
new accident not previously evaluated.
The proposed change does not affect normal plant operations or
configuration, nor does it affect leak rate test methods. The test
history at McGuire (two consecutive successful tests) provides
continued assurance of the leak tightness of the containment
structure.
3. There is no significant reduction in a margin of safety.
The proposed changes are based on NRC-accepted provisions, and
maintain necessary levels of reliability of containment integrity.
The performance-based approach to leakage rate testing recognizes
that historically good results of containment testing provide
appropriate assurance of future containment integrity; this supports
the conclusion that the impact on the health and safety of the
public as a result of extended test intervals is negligible. In
addition, local leak[]rate testing will continue to provide
assurances of overall containment integrity.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: J. Murrey Atkins Library,
University of North Carolina at Charlotte, 9201 University City
Boulevard, North Carolina 28223-0001
Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422
South Church Street, Charlotte, North Carolina 28242
NRC Project Director: Herbert N. Berkow
Entergy Operations Inc., Docket No. 50-382, Waterford Steam
Electric Station, Unit 3, St. Charles Parish, Louisiana
Date of amendment request: October 16, 1996
Description of amendment request: The amendment requests to change
the Waterford 3 Technical Specifications Table 4.3-1 to expand the
applicability for Core Protection Calculator operability and to allow
for the application of a Cycle Independent Shape Annealing Matrix.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
The proposed change will reduce the amount of non-conservatism
presently allowed for linear power level, the CPC delta T power, and
CPC nuclear power signals.
[[Page 6576]]
Changing the tolerance range from plus or minus 2% to between -0.5%
and 10% between 15% and 80% RATED THERMAL POWER, except during
physics testing, will allow more conservative settings than
currently allowed. The consequences of an accident will be reduced
due to the proposed change because it is less likely to be non-
conservative in power.
This proposed change will allow use of Cycle Independent Shape
Annealing Matrix (CISAM) elements. These elements will be validated,
during startup testing, by monitoring the same parameters used for
cycle specific shape annealing matrix (SAM) elements. If the CISAM
is determined to be no longer valid, a cycle specific SAM will be
calculated and used in the CPC's. In addition, use of CISAM gives
better agreement throughout the cycle.
Therefore, the proposed changes will not involve a significant
increase in the probability or consequences of any accident
previously evaluated.
The proposed change to TS power calibration tolerance limits is
conservative relative to the current TS requirement. CPC's cannot
cause an accident and this change will not create the possibility of
a new or different type accident. The changes ensures that the
reactor will trip prior to the current condition due to higher CPC
power.
As stated previously, CISAM modeling removes some of the
uncertainty associated with axial shape and provides increased
assurance that the CPC is appropriately modeling the core.
Therefore, the proposed changes will not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
The proposed change to the TS reduces the amount of non-
conservatism in safety system power indications and maintains the
margin of safety for design basis events which take credit for the
linear power level, the CPC delta T power, and CPC nuclear power
signals.
CISAM will be validated each cycle during startup testing and
must meet the same parameters as cycle specific SAM elements. Since
CISAM has a better accuracy than the cycle dependent SAM, the margin
of safety is improved.
Therefore, the proposed changes will not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of New Orleans
Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L
Street N.W., Washington, D.C. 20005-3502
NRC Project Director: William D. Beckner
GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek
Nuclear Generating Station, Ocean County, New Jersey
Date of amendment request: November 27, 1996
Description of amendment request: The proposed change request would
change the acceptance criteria for the individual cell voltage from
2.0v to 2.09v, change the surveillance frequency for battery specific
gravities to implement the recommendations of IEEE 450-1995, delete
surveillance requirement 4.7.B.4.d, add a clarifying phrase ``while on
a float charge....'' where appropriate, and update the Basis to reflect
these changes.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
This request has been determined to involve No Significant
Hazards in that it does not:
1. Involve a significant increase in the probability or
consequences
of an accident previous[ly] evaluated; (or)
The proposed change in ICVs [individual cell voltages] does not
increase the probability of an accident previously evaluated, as it
increases the required voltage for each ICV.
The proposed change in frequency does not increase the
probability or consequences of an accident previously evaluated, as
the change in the frequency of specific gravity testing is the
result of industry experience gained over the years. The weekly
reading of pilot cell specific gravity and cell voltage, along with
the quarterly reading of all ICVs and a 10% sample of specific
gravities from designated cells provides an acceptable means of
determining cell operability as specified in IEEE 450-1995.
The proposed deletion of Technical Specification Surveillance
Requirement 4.7.B.4.d only removes an unnecessary Technical
Specification surveillance and is consistent with NUREG-1433,
Standard Technical Specifications General Electric Plants, BWR/4,
Revision 1, April 1995. No change to plant systems, components or
operating conditions are associated with this change. Existing
Technical Specification station and diesel generator battery
inspection and testing requirements adequately verify battery
operability and condition.
2. Create the possibility of a new or different kind of accident
from any accident previous[ly] evaluated; (or)
The proposed change does not create the possibility of a new or
different kind of accident than previously evaluated, as the change
only involves raising a required voltage, performing an existing
surveillance on a different frequency, and removing an unnecessary
annunciator surveillance requirement. The station battery and diesel
generator battery low voltage annunciator setpoints do not meet any
of the criteria codified in 10 CFR 50.36 for determining content of
Technical Specifications and removal of surveillance requirement is
consistent with NUREG-1433, Standard Technical Specifications
General Electric Plants, BWR/4, Revision 1, April 1995. There is no
change to hardware or operating conditions.
3. Involve a significant decrease in the margin of safety.
The proposed change to the ICV does not decrease the margin of
safety, as increasing the required voltage actually increases the
margin of safety. The proposed change to the frequency does not
decrease the margin of safety as it continues to require testing and
evaluation of the requisite surveillance points and implements
requirements which have been determined to provide an adequate level
of safety by the IEEE. The removal of Technical Specification
surveillance requirements for the battery low voltage annunciator
setpoints does not affect any plant systems, components or operating
conditions.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: Ocean County Library,
Reference Department, 101 Washington Street, Toms River, NJ 08753
Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw,
Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037
NRC Project Director: Patrick D. Milano, Acting
Northern States Power Company, Docket No. 50-263, Monticello
Nuclear Generating Plant, Wright County, Minnesota
Date of amendment request: January 23, 1997, as revised by letter
dated January 28, 1997.
Description of amendment request: The proposed amendment would make
changes to Section 3.5/4.5.C of the technical specification (TS) bases
to clarify the minimum residual heat removal (RHR) and residual heat
removal service water (RHRSW) pump requirements for post-accident
containment heat removal. In conjunction with the proposed amendment,
the licensee requested NRC staff review and approval of an update to
the design basis accident containment temperature and pressure response
for the limiting single failure (loss of diesel generator) which
results in minimum RHR and RHRSW pump availability.
Basis for proposed no significant hazards determination: As
required by
[[Page 6577]]
10 CFR 50.91(a), the licensee has provided its analysis of the issue of
no significant hazards consideration. The NRC staff has reviewed the
licensee's analysis against the standards of 10 CFR 50.92(c). The NRC
staff's review is presented below.
(1) The proposed changes do not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The proposed amendment will change TS bases to clarify the
minimum RHR and RHRSW pump requirements for post-accident
containment heat removal. The proposed amendment will also correct
an error in a previous analysis on containment temperature and
pressure response following a design basis accident (DBA) that was
submitted for the NRC staff review on May 1, 1986. The proposed
amendment does not affect the physical configuration of the plant or
how it is operated. The licensee's analysis, using a new decay heat
model, determined that the calculated maximum suppression pool
temperature will be 2 degrees Fahrenheit greater (184 degrees
Fahrenheit vs. 182 degrees Fahrenheit) than that predicted in its
previous analysis, based on an earlier decay heat model, that was
submitted for the NRC staff review on May 1, 1986. The licensee
evaluated the effects of this increase on emergency core cooling
system (ECCS) pump net positive suction head, wetwell attached
piping, and environmental conditions in the ECCS pump rooms, and
concluded that the change is acceptable. The consequences or
probability of a previously evaluated accident will, therefore, not
be significantly increased.
(2) The proposed changes do not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
The proposed amendment does not create the possibility of a new or
different kind of accident from any previously evaluated since the
proposed amendment does not affect the physical configuration of the
plant or how it is operated. The proposed amendment revises the TS
bases to clarify the minimum RHR and RHRSW pump requirements for post-
accident containment heat removal.
(3) The proposed changes do not result in a significant
reduction inthe margin of safety.
The proposed amendment will change TS bases to clarify the
minimum RHR and RHRSW pump requirements for post-accident
containment heat removal. The proposed amendment will also correct
an error in a previous analysis on containment temperature and
pressure response following a design basis accident (DBA) that was
submitted for the NRC staff review on May 1, 1986. The proposed
amendment does not affect the physical configuration of the plant or
how it is operated. The licensee's analysis, using a new decay heat
model, determined that the calculated maximum suppression pool
temperature will be 2 degrees Fahrenheit greater (184 degrees
Fahrenheit vs. 182 degrees Fahrenheit) than that predicted in its
previous analysis, based on an ealier decay heat model, that was
submitted for the NRC staff review on May 1, 1986. The licensee
evaluated the effects of this increase on emergency core cooling
system (ECCS) pump net positive suction head, wetwell attached
piping, and environmental conditions in the ECCS pump rooms, and
concluded that the change is acceptable. Therefore, the proposed
amendment does not involve a significant reduction in a margin of
safety.
Based on this review, it appears that the three standards of 10 CFR
50.92(c) are satisfied. Therefore, the NRC staff proposes to determine
that the amendment request involves no significant hazards
consideration.
Local Public Document Room location: Minneapolis Public Library,
Technology and Science Department, 300 Nicollet Mall, Minneapolis,
Minnesota 55401
Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts
and Trowbridge, 2300 N Street, NW. Washington, DC 20037
NRC Project Director: John N. Hannon
Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323,
Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis
Obispo County, California
Date of amendment requests: December 9, 1996
Description of amendment requests: The proposed amendments would
revise the combined Technical Specifications (TS) for the Diablo Canyon
Power Plant (DCPP) Unit Nos. 1 and 2 to revise the surveillance
frequencies from at least once every 18 months to at least once per
refueling interval (nominally 24 months) for the reactor trip system
(RTS) and engineering safety features actuation systems (ESFAS)
instrumentation channels, and make certain changes in trip setpoints
and allowance values due to a setpoint methodology change in support of
the calibration extensions. Channel operational tests (COTs) and trip
actuating device operational tests (TADOTs) associated with these
channels are also being extended. Revisions to the appropriate TS Bases
are being revised to support the TS revisions.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. The proposed change does not involve a significant increase
in the probability or consequences of an accident previously
evaluated.
The proposed TS channel calibration, COT, and TADOT interval
increases from 18 to 24 months, the setpoint change, and the
allowable value changes do not alter the intent or method by which
the channel calibrations are conducted, do not alter the way any
structure, system, or component functions, and do not change the
manner in which the plant is operated. The calibration and
maintenance histories indicate that the equipment will continue to
perform satisfactorily with longer surveillance intervals. With the
exception of the pressurizer water level - high instrument, no
recurring surveillance or maintenance problems were identified for
the RTS or ESFAS instrumentation channels.
The pressurizer water level instruments do not have a safety
limit and are not credited in the DCPP safety analysis. The
recurring surveillance problems were mainly due to calibration zero
shift which is reflected in the statistically determined drift and
in the proposed pressurizer water level high setpoint. The zero
shift problem of these transmitters was a recurring problem with the
calibration procedure. The procedures for calibrating these
instruments have been revised to improve the repeatability of the
surveillance activity.
The trip setpoint and allowable value changes for pressurizer
water level - high are each in the more restrictive direction. The
revised setpoint would tend to trip the reactor sooner than the
present settings. These changes ensure that sufficient margin is
maintained for the pressurizer water level to accommodate the
channel statistical uncertainty resulting from a 30-month operating
cycle.
A statistical analysis of channel uncertainty for a bounding 30-
month operating cycle has been performed. There is sufficient margin
between the existing TS limits and the licensing basis safety
analysis limits to accommodate the channel statistical uncertainty
resulting from a 30-month operating cycle. The existing margin
between the TS limits and the safety analysis limits provides
assurance that plant protective actions will occur as required.
However, a change to the safety analysis limit is proposed in order
to provide additional margin for the RCS loss of [f]low-low
setpoint.
Westinghouse has evaluated the safety analysis limit for the RCS
loss of flow-low setpoint and has determined that the limit can be
changed from 87 percent of MMF to 85 percent of MMF with no impact
on the probability and insignificant impact on the consequences of
accidents already analyzed. The existing conclusions of the DCPP
FSAR Update remain valid with the safety analysis limit change.
Using the new safety analysis limit, sufficient margin exists
between the TS limit and the safety analysis limit to accommodate
the channel statistical uncertainty resulting from a 30-month
operating cycle.
The proposed changes to the allowable values ensure that drift
assumptions regarding the protection racks and direct input
functions are met.
There are no known mechanisms that would significantly degrade
the performance of the evaluated instrument channels during normal
plant operation. All potential time-
[[Page 6578]]
related degradation mechanisms have insignificant effects in the
time frame of interest (maximum of 30 months). PG&E will continue to
perform the maintenance required to maintain the qualification of
this safety related equipment.
Therefore, the proposed changes do not involve a significant
increase in the probability or consequences of an accident
previously evaluated.
2. The proposed change does not create the possibility of a new
or different kind of accident from any accident previously
evaluated.
The proposed pressurizer water level trip setpoint, RCS flow
safety analysis limit, and various allowable value changes provide
adequate margin to accommodate instrument channel uncertainty over a
30-month operating cycle. Plant equipment, which will be set at, or
more conservative than, the trip setpoints, will provide protective
functions to assure that the safety analysis limits are not
exceeded. The change to the RCS loss of flow safety analysis limit
does not create the possibility of a new or different kind of
accident since the setpoint will remain as currently specified and
only results in an insignificant delay in the plant response to the
accident.
Therefore, the proposed change does not create the possibility
of a new or different kind of accident from any accident previously
evaluated.
3. The proposed change does not involve a significant reduction
in a margin of safety.
For almost all the existing DCPP RTS/ESFAS setpoints, the
existing difference between the safety analysis limit and the
setpoints was sufficient to accommodate any changes in instrument
uncertainty.
The change in the pressurizer water level - high setpoint does
not affect a safety analysis limit and, therefore, has no effect on
a margin to safety. Since the normal pressurizer level is maintained
at 60 percent span and the no-load Tavg control level is 22
percent span, a change in the setpoint from less than or equal to 92
percent span to less than or equal to 90 percent span is not
significant to either DCPP plant operation or safety.
The change in the RCS loss of flow-low safety analysis limit
from 87 percent MMF to 85 percent MMF does not affect the existing
plant setpoint and was evaluated to have a negligible effect on the
limiting conditions of a partial loss of flow accident, a single RCP
locked rotor, or RCP shaft break accident. This safety limit change
was also found to have no effect on the DCPP minimum DNBR since the
minimum DNBR is associated with the complete loss of flow accident.
The complete loss of flow accident was evaluated to the Condition II
fault criteria applicable to the partial loss of flow accident
evaluation and was acceptable.
Therefore, the proposed change does not involve a significant
reduction in a margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment requests involve no significant hazards consideration.
Local Public Document Room location: California Polytechnic State
University, Robert E. Kennedy Library, Government Documents and Maps
Department, San Luis Obispo, California 93407
Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and
Electric Company, P.O. Box 7442, San Francisco, California 94120
NRC Project Director: William H. Bateman
Power Authority of The State of New York, Docket No. 50-286, Indian
Point Nuclear Generating Unit No. 3, Westchester County, New York
Date of amendment request: December 23, 1996
Description of amendment request: The proposed amendment would
allow the use of Vantage Plus fuel.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
(1) Does the proposed license amendment involve a significant
increase in the probability or consequences of an accident
previously analyzed?
The probability of occurrence or the consequences of an accident
previously evaluated is not significantly increased. The VANTAGE +
fuel assemblies containing ZIRLOTM clad fuel rods, thimble and
instrument tubes, IFMs, [intermediate fuel mixing assemblies] and
LPD [low-pressure-drop] mid-grids meet the same fuel assembly and
fuel rod design bases as VANTAGE 5 (without IFMs) fuel assemblies in
the other fuel regions. In addition, the 10 CFR 50.46 criteria will
be applied to the ZIRLOTM clad fuel rods, thimble and
instrument tubes, IFM grids, and LPD mid-grids. The use of these
fuel assemblies will not result in a change to the proposed Indian
Point Unit 3 VANTAGE 5 (without IFMs) transition core design and
safety analysis limits. The ZIRLOTM clad material is similar in
chemical composition and has similar physical and mechanical
properties as that of Zircaloy-4. Thus the cladding integrity is
maintained and the structural integrity of the fuel assembly is not
affected. The ZIRLOTM clad fuel rod improves corrosion
resistance and dimensional stability. In addition, the incorporation
of LPD mid-grids and IFMs improves dimensional stability. Since the
dose predictions in the safety analyses are not sensitive to the
fuel assemblies material changes as specified in this report, the
radiological consequences of accidents previously evaluated in the
safety analyses remain valid. Therefore, the probability or
consequences of an accident previously evaluated is not
significantly increased.
(2) Does the proposed license amendment create the possibility
of a new or different kind of accident from any accident previously
evaluated?
The possibility for a new or different type of accident from any
accident previously evaluated is not created, since the VANTAGE +
fuel assemblies containing ZIRLOTM clad fuel rods, thimble, and
instrument tubes, IFMs, and LPD mid-grids will satisfy the same
design bases as that used for VANTAGE 5 (w/o IFMs) fuel assemblies
in the other fuel regions. Since the original design criteria is
being met, the ZIRLOTM clad fuel rods, thimble and instrument
tubes, IFMs, and LPD mid-grids will not be an initiator for any new
accident. All design and performance criteria will continue to be
met and no new single failure mechanisms have been created. In
addition, the use of these fuel assemblies does not involve any
alterations to plant equipment or procedures which would introduce
any new or unique operational modes or accident precursors.
Therefore, the possibility for a new or different kind of accident
from any accident previously evaluated is not created.
(3) Does the proposed amendment involve a significant reduction
in a margin of safety?
The margin of safety is not significantly reduced, since the
VANTAGE + fuel assemblies containing ZIRLOTM clad fuel rods,
thimble and instrument tubes; IFMs, and LPD mid-grids do not change
the proposed Indian Point 3 VANTAGE 5 (w/o IFMs) transition core
design and safety analysis limits. The use of these fuel assemblies
containing fuel rods, thimble and instrument tubes with ZIRLOTM
cladding alloy; IFMs and LPD mid-grids will take into consideration
the normal core operating conditions allowed in the Technical
Specifications. For the transition core and each future cycle reload
core, these fuel assemblies will be specifically evaluated using
standard reload design methods and approved fuel rod design models
and methods. This will include consideration of the core physics
analysis, peaking factors and core average linear heat rate effects.
In addition, the 10 CFR 50.46 criteria will be applied each cycle to
the ZIRLOTM clad fuel rods, thimble and instrument tubes, IFMs,
and LPD mid-grids. Analyses or evaluations will be performed each
cycle to confirm the 10 CFR 50.46 will be met. Therefore, the margin
of safety as defined in the Bases to the Indian Point Unit 3
Technical Specifications and VANTAGE 5 (w/o IFMs) ZIRLOTM
licensing amendment approval is not significantly reduced.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: White Plains Public Library,
100 Martine Avenue, White Plains, New York 10601.
Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle,
New York, New York 10019.
NRC Project Director: S. Singh Bajwa, Acting
[[Page 6579]]
TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak
Steam Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: July 9, 1996 (TXX-96393)
Brief description of amendments: The proposed changes would
increase the minimum allowable value of the Unit 1 Steam Line Pressure-
-Low Safety Injection and Steam Line Isolation functions. These changes
are needed to ensure that the instrumentation error is properly
accounted for in the Technical Specifications.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
The changes in the License Amendment Request proposes more
restrictive setpoint Allowable Values for the Steam Line pressure--
Low channels of the Engineered Safety Features Actuation System
(ESFAS). These more restrictive values assure that all applicable
safety analysis limits are being met. Changing an Allowable Value in
the Technical Specifications has no impact on the probability of
occurrence of any accident previously evaluated. None of the
accident analyses were affected, therefore, the consequences of all
previously evaluated accidents remain unchanged.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any accident previously evaluated?
The proposed changes involve the use of a more conservative
value for the Allowable Value for the Steam Line Pressure--Low
Safety Injection and Steam Line Isolation functions. As such, none
of the changes effect plant hardware or the operation of plant
systems in a way that could initiate an accident. Therefore, the
proposed changes do not create the possibility of a new or different
kind of accident from any accident previously evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
There were no changes made to any of the accident analyses or
safety analysis limits as a result of this proposed change. Further,
the proposed change does not affect the acceptance criteria for any
analyzed event. ESFAS will remain capable of performing its safety
function, and the new requirement will continue to provide adequate
assurance of that capability. Making the Allowable Value more
restrictive provides increased assurance that the channels will
function within the safety analysis limits assumed in the safety
analyses. The margin of safety established by the Limiting
Conditions for Operation also remains unchanged. Thus there is no
effect on the margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of Texas at
Arlington Library, Government Publications/Maps, 702 College, P.O. Box
19497, Arlington, TX 76019
Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and
Bockius, 1800 M Street, N.W., Washington, DC 20036
NRC Project Director: William D. Beckner
TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak
Steam Electric Station, Units 1 and 2, Somervell County, Texas
Date of amendment request: July 10, 1996 (TXX-96405), as
supplemented by letter dated October 1, 1996 (TXX-96475)
Brief description of amendments: The proposed change would take
credit for the addition of train oriented Fan Coil Units for each UPS &
Distribution Room and would provide redundancy to the existing Air
Conditioning Units.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
1. Do the proposed changes involve a significant increase in the
probability or consequences of an accident previously evaluated?
The UPS HVAC System is a support system for other safety related
equipment, primarily the Uninterruptible Power Supplies and some of
their distribution equipment. The only impact that this system can
have on the probability or consequences of an accident must result
from the failure of the system to provide adequate support to the
supported safety related equipment when that supported safety
related equipment is required to operate.
Allowing same train cooling to satisfy the LCO is considered
equivalent to the existing Technical Specification. The proposed
changes allow the use of the same train UPS Room Fan Coil Units or
the same train UPS A/C Train to support a UPS & Distribution Room.
Surveillance requirements are added or modified to ensure that
the credited support equipment will be available when needed.
Unnecessary starts of the UPS A/C Trains have been eliminated from
the specifications. Overall, this is considered an enhancement that
will increase the reliability of the UPS HVAC Systems. Because both
the existing specification and the proposed revision to the
specification continue to ensure normal support and the availability
of at least one train of equipment in the event of a design basis
accident, with the same or increased reliability, the consequences
of an accident previously evaluated is not affected.
Changing the specification from a ``common'' specification which
impacts both units simultaneously to a specification which applies
to both units separately is basically just an administrative change.
Having ``common'' specifications is an aid to the operator to
provide an alert that both units are affected. With the new LCO,
both units may not be affected because rooms may now be cooled
separately. Because both CPSES Units remain properly covered,
however, this change will not significantly increase the probability
of consequences of an accident.
The revision to the existing ACTION is considered equivalent
except for the change of the Allowed Outage Time (AOT) from seven
days to 30 days. This change is based on the significance of the
heating and cooling function but does represent an increase in AOT
and thus an increase in the probability that the supported functions
could be unavailable. This increase is not considered significant
based on the following several factors:
a)the systems design is based on a conservative assessment of
the worst postulated conditions in the rooms;
b) generally, less than design cooling is required and a short
duration or partial failure may have little or no impact on the
systems ability to perform its function;
c) the multiple backups available (two UPS A/C Trains and only
one UPS Room Fan Coil Unit per each room) increase the potential of
restoring additional cooling if needed;
d) the ability to perform alternate actions if normal cooling is
lost such as circulating air via existing fans or portable fans
thereby extending the time before cooling must be restored; and
e) the extended AOT would allow more time and opportunity to
perform corrective maintenance to ensure high equipment reliability.
The new ACTION for loss of cooling reflects requirements that
already exist in the Technical Specifications. The AOT for this
ACTION statement is 72 hours which is based on the risk from an
event occurring requiring the inoperable UPS A/C Train, and the
remaining UPS Room Fan Coil Units and A/C Train fans providing the
required protection.
The new ACTION for loss of cooling and ventilation reflects a
conservative response to the potential impact of such a condition.
The proposed AOT is one hour. One hour is based on the time lag
available from the operating temperature to the maximum Technical
Specification limit of the UPS & Distribution Rooms. The addition of
a specific ACTION in lieu of relying on Specification 3.0.3,
although essentially equivalent, is consistent with the methodology
of the improved Standard Technical Specifications and alerts the
operator to the significance of the situation.
The changes made to the surveillance ensure that the UPS Room
Fan Coil Units will operate. The UPS Room Fan Coil Units are
connected to the emergency busses and TS 4.8.1.1.2f. demonstrates
the energization of emergency busses with permanently connected
loads. The changes made to the 18
[[Page 6580]]
month surveillances on the UPS A/C trains were changed from the
Safety Injection signal with the Blackout Test signal to ``...
actual or simulated actuation signal''. This is consistent with
NUREG-1431, ``Standard Technical Specifications Westinghouse
Plants''.
The changes to the BASES are descriptive in nature to reflect
the other changes and by themselves have no impact on the
probability or consequences of an accident.
The ability to cope with station blackout and design basis fires
is maintained or enhanced. For station blackout coping, the UPS A/C
fans are considered to remain available while additional cooling is
provided by a single available Fan Coil Unit.
In summary, the proposed changes take advantage of the increased
reliability offered by the revised system design. It also maintains
the level of support provided by the system while at worst, allowing
a slight decrease in availability (in certain situations) which is
not considered significant. As a result, it is concluded that none
of the changes made to the existing Technical Specification involve
a significant increase in the probability or consequences of an
accident previously evaluated.
2. Do the proposed changes create the possibility of a new or
different kind of accident from any previously evaluated?
Revising this specification to take credit for the new UPS Room
Fan Coil Units, to take credit for same train UPS A/C Train support
for a UPS and Distribution Room, to make the specification unit
specific instead of common, to make the surveillances appropriate
for the credited equipment, and to make the action statements
appropriate for the credited equipment and their significance, does
not by itself alter plant hardware. Plant procedures are only
altered to the extent that the revised specification will allow
different configurations of equipment in the UPS HVAC System to be
operated at different times. These changes ensure continued support
of the safety related equipment in the affected areas and do not
affect the equipments failure or failure modes. As a result, these
changes to the Technical Specification do not create the possibility
of a new or different kind of accident from any previously
evaluated.
3. Do the proposed changes involve a significant reduction in a
margin of safety?
None of the changes being proposed alter the environmental
conditions which are to be maintained in the areas supported by an
OPERABLE UPS HVAC System during normal operations and following an
accident. As a result, the margin of safety for these functions
remains the same. The only potential adverse impact is the system's
postulated availability, as discussed in the response to question 1
above. This reduction in availability is to a great extent mitigated
by the projected increase in system reliability. As noted in the
response to question 1, there is no significant impact on the
accident analyses. Thus, even if system availability issues were
considered an aspect of margin of safety, the proposed changes do
not involve a significant reduction in margin of safety.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 10 CFR 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: University of Texas at
Arlington Library, Government Publications/Maps, 702 College, P.O. Box
19497, Arlington, TX 76019
Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and
Bockius, 1800 M Street, N.W., Washington, DC 20036
NRC Project Director: William D. Beckner
Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339,
North Anna Power Station, Units No. 1 and No. 2, Louisa County,
Virginia
Date of amendment request: December 17, 1996
Description of amendment request: The proposed changes will allow
one of the two service water loops to be isolated from the component
cooling water heat exchangers (CCHXs) during power operation in order
to refurbish sections of the isolated service water headers. The
proposed temporary changes will be valid for two periods of up to 35
days each for implementation of the service water upgrades associated
with the repair of the sections of the 24-inch service water supply and
return piping to/from the CCHXs.
Basis for proposed no significant hazards determination: As
required by 10 CFR 50.91(a), the licensee has provided its analysis of
the issue of no significant hazards consideration, which is presented
below:
Specifically, operation of North Anna Power Station in
accordance with the proposed Technical Specifications changes will
not:
1. Involve a significant increase in the probability or
consequences of an accident previously evaluated.
The piping refurbishment project and the proposed temporary
changes to the SW [service water] and CC [component cooling]
Technical Specifications have been evaluated to assess their impact
on the normal operation of the SW and CC systems and to ensure that
the design basis safety functions of each system are preserved. The
SW system is required to function during all normal and emergency
operating conditions. During normal plant operation, the SW system
provides cooling water to the CCHXs, charging pump coolers,
instrument air compressor coolers, and control room chiller
condensers of both units. Within the first 168 hour Section 3/
4.7.4.1.d TS AS [Action Statement] of isolation of the header which
is to be repaired, temporary 10'' diameter SW lines (one supply and
one return) will be installed to supply the SW to the charging pumps
coolers, instrument air compressors coolers, Unit 2 CR chillers and
spent fuel pool (SFP) coolers to satisfy design basis conditions.
These temporary lines will be routed from the operating part of the
36'' SW headers while the 24'' headers to CCHXs are being repaired.
The temporary lines will be dismantled when the repaired header is
returned to operation (second 168 hour AS). During the two 35-day
periods, one header will operate with its 24-inch piping to/from the
CCHXs temporarily blanked. To avoid operation of the SW pump at
abnormal conditions (low flow) on this ``partially deadlocked''
header, a temporary cross-connect will be installed to by-pass the
CCHXs.
SW system operation with the cross-connect installed was
evaluated for design basis accident (DBA) conditions. The DBA
condition for the SW system is a loss-of-coolant accident on one
unit with simultaneous loss-of-offsite-power to both units. [An] SW
system hydraulic analysis has been performed to verify that adequate
flow is provided to the containment recirculation spray heat
exchangers (RSHXs) with the temporary cross-connect installed and
throttled open, assuming the occurrence of the most limiting single
failure. Therefore, there is no increase in probability or
consequences of the DBA condition.
Utilizing only one SW header to supply flow to the CCHXs has the
potential to affect the reliability of the CC system and all of the
equipment cooled by CC. A review of the equipment affected by this
phase of the SW restoration project was performed to evaluate the
impact on initiating event frequency. Since the SW system and CC
system are support systems used to remove heat, a failure in either
of these systems does not affect the initiating event frequency of
any design basis event. Additionally, an estimate of the impact on
core damage frequency is provided below. The impact on the North
Anna Probabilistic Safety Assessment (PSA) during implementation of
this DCP [design change package] is similar to impact of work
performed under DCP-94-010 since the scope of work of both DCPs is
repair/replacement of different portions of the same 24'' SW headers
to CCHXs. The only difference from a PSA standpoint is that CDF
[core damage frequency] for DCP-94-010 was calculated based on 140
days supply of CCHXs from one SW header while per this DCP it is
only 70 days. Therefore, results of PSA evaluation for DCP-94-010
are conservatively applied to this DCP. The activities to be
performed during the refurbishment project and the various system
alignments required have been evaluated using the Individual Plant
Examination (IPE) Probabilistic Safety Assessment (PSA) model for
North Anna Power Station. This model is used in a manner that is
generally consistent with the Electric Power Research Institute
(EPRI) PSA Applications Guide TR-105396. The effect on the PSA model
is a slight increase in the frequency of reactor trips and an
increase in the probability of RHR [residual heat removal] failure.
The increased frequency of reactor trips is due to the decreased
reliability of the CC system to supply cooling to the RCP [reactor
coolant pump] motor. When only one SW header is available to the CC
heat exchangers
[[Page 6581]]
the frequency of losing this single header is dominated by the
probability of both SW pumps failing. Also considered was the
frequency of pipe rupture anywhere in the single available header.
When the single SW header fails to supply cooling to the CC heat
exchangers, the CC system will heatup causing inadequate cooling for
sustained operation of the RCPs. Tripping these pumps results in a
reactor trip. The second SW header can be expected to supply other
equipment with cooling. This scenario is appropriately modeled as a
reactor trip with main feedwater available initiating event. A
sensitivity analysis shows the increase in CDF to be about 1E-8/
year. The total effect of this DCP includes a failure analysis of
the reactor coolant pump and motor in case of loss of CCW.
The CC system is also included in the PSA model as a support
system for RHR cooling. The RHR system is used to reduce reactor
coolant system temperatures from 350 deg.F (hot shutdown) to
140 deg.F (cold shutdown). The only accident initiator that requires
the unit to be cooled down and placed on RHR cooling are sequences
which are initiated with a steam generator tube rupture. (Note that,
for the North Anna plant design, RHR is separate from the safety
injection system and the low head safety injection pumps.) The
increased probability for the loss of RHR when only one SW header is
available to the CCHXs is estimated using fault tree analysis and is
dominated by the failure of both SW pumps. The probability for the
loss of both SW pumps aligned to the CCHXs is estimated to be 1.5E-
4. The effect of this increase in RHR failure probability was
determined by adding this probability to the top single event in the
RHR function and recalculating the new CDF. The resulting increase
in CDF as a result of RHR system failure following a steam generator
tube rupture is less than 1E-8 per year.
The CC system is further included in the PSA model as part of
the loss of RCP seal cooling as an initiating event and as a loss of
function during other initiating event scenarios. The effect on the
probability for a loss of RCP seal cooling due to losing CC cooling
to the RCP thermal barriers is negligible due to the high
reliability of the charging system to provide seal injection.
The total effect of this DCP on core damage frequency (CDF) was
estimated by a sensitivity analysis combining both the change in the
reactor trip initiating event frequency and the increased failure
probability of RHR. It was evaluated that during implementation of
this DCP, CCHXs will be supplied from one SW header for 70 days (35
x 2=70), therefore, the increase in CDF previously evaluated in DCP-
94-010 based on 140 days is conservative. This DCP does not affect
the containment systems and there would not be any significant
change in off-site dose since the containment heat removal portion
of the SW system is not affected and the increase in CDF is
insignificant. The small increase in CDF calculated for the repair
activities and the procedure developed to provide contingency
actions result in the conclusion that this work does not represent a
significant increase in core damage frequency.
2. Create the possibility of a new or different kind of accident
from any accident previously evaluated.
The proposed changes to the allowed outage time only provide
operational flexibility needed to perform necessary repairs. During
the project, there will be a significant time period when all the
CCHXs are aligned to one SW loop. The possibility of an interruption
of SW supply to the heat exchangers during a DBA is eliminated by
defeating the closure of the 24-inch SW isolation MOVs [motor-
operated valves] to the CCHXs on [an] SI/CDA [safety injection/
containment depressurization actuation] signal. Both SW headers will
be available for equipment required for safe shutdown of the units
(i.e., RSHXs, charging pumps, and CR/ESGR [control room/emergency
switchgear room] chillers). The SW pipe repair activities and the
installation/removal of the SW cross-connect and temporary piping do
not create the possibility for a malfunction of equipment different
than previously evaluated. Results of the Johnston Pump NPSH [net
positive suction head] test proved to be satisfactory for the
anticipated SW pump flow rates under modes of station operation for
this project, therefore, the possibility for an accident of a
different type than was previously evaluated in the Safety Analysis
Report will not be created. Based on the above, implementation of
the restoration project and approval of the proposed Technical
Specifications changes will not introduce any new accident
initiators nor affect the performance of accident mitigation
systems.
3. Involve a significant reduction in a margin of safety.
The proposed changes to the schedule only provide operational
flexibility to perform the required SW pipe refurbishment. The
Technical Specifications continue to require the SW and CC systems
to remain functional during the period with a single SW supply to
the CCHXs. As stated in item (1) above, the SW system is fully
capable of performing its DBA function during the course of the pipe
refurbishment project with the proposed Technical Specification
changes in place. The effect of this pipe refurbishment project on
CC system reliability was estimated by a sensitivity analysis
combining both the change in the reactor trip initiating event
frequency and the increased failure probability of RHR resulting in
about a 1E-8 per year increase in CDF. Since this project will not
affect the containment systems, there would not be any significant
change in off-site dose, except that resulting directly from the
slight increase in CDF.
The NRC staff has reviewed the licensee's analysis and, based on
this review, it appears that the three standards of 50.92(c) are
satisfied. Therefore, the NRC staff proposes to determine that the
amendment request involves no significant hazards consideration.
Local Public Document Room location: The Alderman Library, Special
Collections Department, University of Virginia, Charlottesville,
Virginia 22903-2498.
Attorney for licensee: Michael W. Maupin, Esq., Hunton and
Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond,
Virginia 23219.
NRC Project Director: F. Mark Reinhart (Acting)
Notice of Issuance of Amendments To Facility Operating Licenses
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application complies
with the standards and requirements of the Atomic Energy Act of 1954,
as amended (the Act), and the Commission's rules and regulations. The
Commission has made appropriate findings as required by the Act and the
Commission's rules and regulations in 10 CFR Chapter I, which are set
forth in the license amendment.
Notice of Consideration of Issuance of Amendment to Facility
Operating License, Proposed No Significant Hazards Consideration
Determination, and Opportunity for A Hearing in connection with these
actions was published in the Federal Register as indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.12(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) the
applications for amendment, (2) the amendment, and (3) the Commission's
related letter, Safety Evaluation and/or Environmental Assessment as
indicated. All of these items are available for public inspection at
the Commission's Public Document Room, the Gelman Building, 2120 L
Street, NW., Washington, DC, and at the local public document rooms for
the particular facilities involved.
Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318,
Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert
County, Maryland
Date of application for amendments: September 10, 1996
Brief description of amendments: The amendments extend the
automatic actuation logic channel functional test interval of the
Engineering Safety
[[Page 6582]]
Features Actuation System and the surveillances test interval of the
containment sump isolation valves from monthly to quarterly.
Date of issuance: January 23, 1997
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment Nos.: 218 and 195
Facility Operating License Nos. DPR-53 and DPR-69: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: October 9, 1996 (61 FR
52963) The Commission's related evaluation of these amendments is
contained in a Safety Evaluation dated January 23, 1997 No significant
hazards consideration comments received: No
Local Public Document Room location: Calvert County Library, Prince
Frederick, Maryland 20678.
Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle
County Station, Units 1 and 2, LaSalle County, Illinois
Date of application for amendments: October 31, 1996
Brief description of amendments: The amendments relocate the
requirements for seismic monitoring instrumentation from Technical
Specification (TS) 3/4.3.7.2, ``Seismic Monitoring Instrumentation'' to
licensee-controlled documents in accordance with Generic Letter 95-10,
``Relocation of Selected Technical Specifications Requirements Related
to Instrumentation.'' The amendments also add a condition to the
operating licenses which approves the relocation of the TS requirements
to the UFSAR.
Date of issuance: January 29, 1997 Effective date: Immediately, to
be implemented within 90 days.
Amendment Nos.: 117, 102
Facility Operating License Nos. NPF-11 and NPF-18: The amendments
revised the Technical Specifications and the license.
Date of initial notice in Federal Register: December 18, 1996 (61
FR 66703) The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 29, 1997. No significant
hazards consideration comments received: No
Local Public Document Room location: Jacobs Memorial Library,
Illinois Valley Community College, Oglesby, Illinois 61348.
Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley
Power Station, Unit No. 1, Shippingport, Pennsylvania
Date of application for amendment: September 9, 1996, as
supplemented December 20, 1996
Brief description of amendment: The amendment revises the Minimum
Channels Operable requirement of Item 4.c (Steam Line Isolation,
Containment Pressure Intermediate--High-High) of Technical
Specification (TS) Table 3.3-3 from 3 channels to 2 channels provided
the provisions of Action Statement 14 are followed. This change makes
this Beaver Valley Power Station, Unit No. 1 TS consistent with the
comparable Beaver Valley Power Station, Unit No. 2 TS. The amendment
also revises the minimum charging pump discharge pressure in TS 3/4.5.5
and associated Bases from 2311 psig to 2397 psig. This change ensures
that safety analysis assumptions for safety injection flow are met.
Date of issuance: January 27, 1997
Effective date: As of date of issuance, to be implemented within 60
days.
Amendment No: 201
Facility Operating License No. DPR-66. Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: October 23, 1996 (61 FR
55032) The supplemental letter provided clarifying information that did
not change the initial proposed no significant hazards consideration
determination or the original notice. The Commission's related
evaluation of the amendment is contained in a Safety Evaluation dated
January 27, 1997. No significant hazards consideration comments
received: No
Local Public Document Room location: B. F. Jones Memorial Library,
663 Franklin Avenue, Aliquippa, PA 15001
Illinois Power Company and Soyland Power Cooperative, Inc., Docket
No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County,
Illinois
Date of application for amendment: August 15, 1996, and as
supplemented by letters dated October 28, November 15, 1996, and
January 7, 1997.
Brief description of amendment: The amendment changes the Clinton
Power Station (CPS) Technical Specifications to incorporate the revised
Safety Limit Minimum Critical Power Ratio (SLMCPR) as calculated by
General Electric (GE) for CPS Cycle 7. The need to change the SLMCPR
resulted from the 10 CFR Part 21 condition reported by GE in their
letter to the NRC dated May 24, 1996.
Date of issuance: January 22, 1997
Effective date: January 22, 1997
Amendment No.: 113
Facility Operating License No. NPF-62: The amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: September 11, 1996 (61
FR 47978). The licensee's letters of October 28, November 15, 1996, and
January 7, 1997, provided clarifying information and did not make
significant changes to the initial Federal Register notice. The
Commission's related evaluation of the amendment is contained in a
Safety Evaluation dated January 22, 1997. No significant hazards
consideration comments received: No
Local Public Document Room location: The Vespasian Warner Public
Library, 120 West Johnson Street, Clinton, Illinois 61727
Northeast Nuclear Energy Company, Docket No. 50-245, Millstone
Nuclear Power Station, Unit 1, New London County, Connecticut
Date of application for amendment: August 29, 1996
Brief description of amendment: The amendment revises the Technical
Specifications to (1) modify the applicability requirements for certain
radiation monitors so that the radiation monitors are required to be
operable only when secondary containment integrity is required to be
operable; (2) delineate when secondary containment integrity is
required; (3) modify standby gas treatment operability requirements;
(4) make editorial corrections to clarify the configuration of the
radiation monitors; and (5) revise the associated Bases sections.
Date of issuance: January 14, 1997
Effective date: As of the date of issuance, to be implemented
within 30 days.
Amendment No.: 98
Facility Operating License No. DPR-21: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: October 17, 1996 (61 FR
54242) The Commission's related evaluation of the amendment is
contained in a Safety Evaluation dated January 14, 1997 No significant
hazards consideration comments received: No.
Local Public Document Room location: : Learning Resources Center,
Three Rivers Community-Technical College, 574 New London Turnpike,
Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49
Rope Ferry Road, Waterford, CT 06385
[[Page 6583]]
Philadelphia Electric Company, Docket Nos. 50-352 and 50-353,
Limerick Generating Station, Units 1 and 2, Montgomery County,
Pennsylvania
Date of application for amendments: June 28, 1996, as supplemented
by letters dated November 4 and 5, and December 9, 1996
Brief description of amendments: These amendments revise the
technical specifications to incorporate performance-based testing, in
accordance with 10 CFR Part 50, Appendix J, ``Primary Reactor
Containment Leakage Testing For Water-Cooled Power Reactors,'' Option
B. This option allows utilities to extend the frequencies of the Type A
Containment Leak Rate Test, and Type B and C Local Leak Rate Tests
based on the performance and design of the containment and components.
Date of issuance: January 24, 1997
Effective date: Both units, as of date of issuance and shall be
implemented within 30 days.
Amendment Nos.: 118 and 81
Facility Operating License Nos. NPF-39 and NPF-85. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: October 23, 1996 (61 FR
55038) The supplemental letters provided clarifying information that
did not change the initial proposed no significant hazards
consideration determination or the original notice. The Commission's
related evaluation of the amendments is contained in a Safety
Evaluation dated Janaury 24, 1997. No significant hazards consideration
comments received: No
Local Public Document Room location: Pottstown Public Library, 500
High Street, Pottstown, PA 19464
Philadelphia Electric Company, Docket Nos. 50-352 and 50-353,
Limerick Generating Station, Units 1 and 2, Montgomery County,
Pennsylvania
Date of application for amendments: May 20, 1996
Brief description of amendments: These amendments revise Technical
Specifications (TS) Sections 3/4.4.9.2, 3/4.9.11.1, 3/4.9.11.2, and the
associated TS Bases 3/4.4.9 and 3/4.9.11, to more clearly describe that
the Residual Heat Removal (RHR) system Shutdown Cooling mode of
operation consists of four ``subsystems.'' These TS sections pertain to
plant operations during Operational Conditions (OPCONs) 4, ``Cold
Shutdown'' and 5, ``Refueling.'' In addition, the proposed TS change
would make administrative changes to TS Section 3/4.4.9.1 to ensure
consistency in terminology regarding the description of Shutdown
Cooling ``subsystems.'' The proposed TS changes are consistent with the
guidance delineated in the Improved TS (i.e., NUREG-1433, Revision 1,
``Standard Technical Specifications General Electric Plants, BWR/4,''
dated April 1995) which indicates that the RHR Shutdown Cooling mode of
operation is comprised of two loops and four subsystems (i.e., two
subsystems per loop).
Date of issuance: January 28, 1997
Effective date: As of date of issuance and shall be implemented
within 30 days.
Amendment Nos.: 119 and 82
Facility Operating License Nos. NPF-39 and NPF-85. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: October 23, 1996 (61 FR
55036) The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 28, 1997. No significant
hazards consideration comments received: No
Local Public Document Room location: Pottstown Public Library, 500
High Street, Pottstown, PA 19464
Philadelphia Electric Company, Docket No. 50-353, Limerick
Generating Station, Unit 2, Montgomery County, Pennsylvania
Date of application for amendment: August 5, 1996, as supplemented
December 4, 1996
Brief description of amendment: The amendment revised TS Section
2.1 and its associated TS Bases to reflect the change in the Minimum
Critical Power Ratio Safety Limit due to the plant specific evaluation
performed by General Electric Company (GE), for Limerick Generating
Station, Unit 2, Cycle 4.
Date of issuance: January 29, 1997
Effective date: As of date of issuance and shall be implemented
within 30 days
Amendment No.: 83
Facility Operating License No. NPF-85. This amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: November 6, 1996 (61 FR
57491) The December 4, 1996, letter provided clarifying information
that did not change the initial proposed no significant hazards
consideration determination or the initial notice. The Commission's
related evaluation of the amendment is contained in a Safety Evaluation
dated January 29, 1997. No significant hazards consideration comments
received: No
Local Public Document Room location: Pottstown Public Library, 500
High Street, Pottstown, PA 19464
Philadelphia Electric Company, Docket Nos. 50-352 and 50-353,
Limerick Generating Station, Units 1 and 2, Montgomery County,
Pennsylvania
Date of application for amendments: March 29, 1996, as supplemented
by letters dated December 5, 1996, and January 15, 1997
Brief description of amendments: These amendments modify Technical
Specification (TS) Section 4.5.1.d.2.b to delete the requirement to
perform in-situ functional testing of the Automatic Depressurization
System (ADS) valves once every 24-months as part of start-up testing
activities.
Date of issuance: January 29, 1997
Effective date: Both units, as of date of issuance, to be
implemented within 30 days.
Amendment Nos.: 120 and 84
Facility Operating License Nos. NPF-39 and NPF-85. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: November 6, 1996 (61 FR
57488) The December 5, 1996, and January 15, 1997, letters provided
clarifying information that did not change the initial proposed no
significant hazards consideration determination nor the initial notice.
The Commission's related evaluation of the amendments is contained in a
Safety Evaluation dated January 29, 1997. No significant hazards
consideration comments received: No
Local Public Document Room location: Pottstown Public Library, 500
High Street, Pottstown, PA 19464
Power Authority of The State of New York, Docket No. 50-286, Indian
Point Nuclear Generating Unit No. 3, Westchester County, New York
Date of application for amendment: October 1, 1996
Brief description of amendment: The amendment allows for a one-time
extension of the surveillance intervals for the containment isolation
valve seat leakage test, the isolation valve seal water test, the boron
injection tank leakage test, the containment spray nozzle test, and the
city water backup to the auxiliary boiler feed pump test.
Date of issuance: January 28, 1997
Effective date: As of the date of issuance to be implemented within
30 days.
Amendment No.: 172
Facility Operating License No. DPR-64: Amendment revised the
Technical Specifications.
Date of initial notice in Federal Register: December 4, 1996 (61 FR
[[Page 6584]]
64393) The Commission's related evaluation of the amendment is
contained in a Safety Evaluation dated January 28, 1997 No significant
hazards consideration comments received: No
Local Public Document Room location: White Plains Public Library,
100 Martine Avenue, White Plains, New York 10610.
Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments: October 1, 1996, supplemented
October 31, 1996
Brief description of amendments: The amendments change Technical
Specifications 3/4.7.1.5, ``Main Steam Line Isolation Valves (MSIVs),''
and 3/4.3.2, ``Engineered Safety Feature Actuation System
Instrumentation.'' The amendments accommodate entry into Modes 3 and 2
prior to performing MSIV closure time testing in Mode 2, allow
additional time for the repair and testing of inoperable MSIVs in
certain operating Modes, delete footnotes that are no longer
applicable, and change the low steam line pressure trip setpoint value
for safety injection, turbine trip and feedwater isolation to make it
consistent with the actual plant configuration.
Date of issuance: January 17, 1997
Effective date: Both units, as of date of issuance, to be
implemented prior to entry into Mode 3 from the current outage.
Amendment Nos. 187 and 170
Facility Operating License Nos. DPR-70 and DPR-75. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: October 23, 1996 (61 FR
55040) The supplemental letter changed the TSs to provide greater
consistency with requirements of NUREG-1431 ``Standard Technical
Specifications - Westinghouse Plants,'' Revision 1, and did not change
the initial proposed no significant hazards consideration determination
or the Federal Register notice. The Commission's related evaluation of
the amendments is contained in a Safety Evaluation dated January 17,
1997. No significant hazards consideration comments received: No
Local Public Document Room location: Salem Free Public Library, 112
West Broadway, Salem, NJ 08079
Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments: October 24, 1996, as
supplemented December 23, 1996
Brief description of amendments: The amendments changed Technical
Specification 3/4.7.1.2, ``Auxiliary Feedwater System.'' The changes
revised the 18-month surveillance performed on the system's pumps and
valves because testing of the turbine driven Auxiliary Feedwater pump
can only be performed in higher modes when there is sufficient
secondary steam pressure.
Date of issuance: January 23, 1997
Effective date: As of date of issuance, to be implemented within 30
days
Amendment Nos. 188 and 171
Facility Operating License Nos. DPR-70 and DPR-75. The amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: November 19, 1996 (61
FR 58905) The December 23, 1996, letter proposed changes to TS 3/4.3.2
to provide consistency with those proposed in the October 24, 1996,
letter and therefore did not change the initial proposed no significant
hazards consideration determination and was within the scope of the
initial notice. The Commission's related evaluation of the amendments
is contained in a Safety Evaluation dated January 23, 1997. No
significant hazards consideration comments received: No
Local Public Document Room location: Salem Free Public Library, 112
West Broadway, Salem, NJ 08079
Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem
County, New Jersey
Date of application for amendments: September 25, 1996
Brief description of amendments: The amendments relocate the list
of containment isolation valves from the Technical Specifications to
the Salem Updated Final Safety Analysis Report and correct references.
Date of issuance: January 30, 1997
Effective date: Both units, as of date of issuance, to be
implemented within 60 days.
Amendment Nos. 189 and 172
Facility Operating License Nos. DPR-70 and DPR-75. The amendments
revised the Technical Specifications and the License.
Date of initial notice in Federal Register: October 23, 1996 (61 FR
55039) The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 30, 1997. No significant
hazards consideration comments received: No
Local Public Document Room location: Salem Free Public Library, 112
West Broadway, Salem, NJ 08079
Virginia Electric and Power Company, et al., Docket Nos. 50-338 and
50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa
County, Virginia
Date of application for amendments: January 31, 1996, as revised
November 26, 1996. The November 26, 1996, submittal withdrew the
proposed change to surveillance tests being performed at power.
Brief description of amendments: These amendments will revise the
minimum emergency diesel generator day tank fuel oil volume.
Date of issuance: January 17, 1997
Effective date: January 17, 1997
Amendment Nos.: 203 and 184
Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised
the Technical Specifications.
Date of initial notice in Federal Register: February 28, 1996 (61
FR 7559) The Commission's related evaluation of the amendments is
contained in a Safety Evaluation dated January 17, 1997. No significant
hazards consideration comments received: No.
Local Public Document Room location: : The Alderman Library,
Special Collections Department, University of Virginia,
Charlottesville, Virginia 22903-2498.
Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301,
Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks,
Manitowoc County, Wisconsin
Date of application for amendments: February 8, 1996, as
supplemented August 15, December 2 and December 19, 1996, and January
6, 1997
Brief description of amendments: These amendments revise Technical
Specification (TS) Section 15.3.10, ``Control Rod and Power
Distribution Limits,'' to improve the clarity of this section and add
surveillance requirements to Section 15.4.1, ``Operational Safety
Review.''
Date of issuance: January 16, 1997
Effective date: January 16, 1997, with full implementation within
45 days
Amendment Nos.: Unit 1 - 171, Unit 2 - 175
Facility Operating License Nos. DPR-24 and DPR-27: Amendments
revised the Technical Specifications.
Date of initial notice in Federal Register: March 13, 1996 (61 FR
10398) The August 15, December 2 and
[[Page 6585]]
December 19, 1996, and January 6, 1997, letters provided clarifying
information and updated TS pages that were within the scope of the
original application and did not change the NRC staff's initial
proposed no significant hazards consideration determination. The
Commission's related evaluation of the amendments is contained in a
Safety Evaluation dated January 16, 1997. No significant hazards
consideration comments received: No.
Local Public Document Room location: Joseph P. Mann Library, 1516
Sixteenth Street, Two Rivers, Wisconsin 54241
Previously Published Notices Of Consideration Of Issuance Of
Amendments To Facility Operating Licenses, Proposed No Significant
Hazards Consideration Determination, And Opportunity For A Hearing
The following notices were previously published as separate
individual notices. The notice content was the same as above. They were
published as individual notices either because time did not allow the
Commission to wait for this biweekly notice or because the action
involved exigent circumstances. They are repeated here because the
biweekly notice lists all amendments issued or proposed to be issued
involving no significant hazards consideration.
For details, see the individual notice in the Federal Register on
the day and page cited. This notice does not extend the notice period
of the original notice.
Florida Power and Light Company, Docket Nos. 50-250 and 50-251,
Turkey Point, Units 3 and 4, Dade County, Florida
Date of amendment request: December 17, 1996
Description of amendment request: The proposed amendments would
modify the Turkey Point Units 3 and 4 Technical Specifications to
change the Reactor Coolant Pump (RCP) flywheel surveillance
requirement. The proposed change will require RCP flywheel inspections
once every ten years.
Date of publication of individual notice in Federal Register:
January 10, 1997 (62 FR 1476)
Expiration date of individual notice: February 10, 1997
Local Public Document Room location: Florida International
University, University Park, Miami, Florida 33199
Illinois Power Company and Soyland Power Cooperative, Inc., Docket
No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County,
Illinois
Date of amendment request: December 13, 1996
Description of amendment request: The proposed amendment would
approve transfer of Soyland Power Cooperative's 13.21% minority
ownership interest in the Clinton Power Station to Illinois Power
Company. This action would result in Illinois Power Company becoming
the sole owner of the Clinton Power Station.
Date of publication of individual notice in Federal Register:
January 29, 1997 (62 FR 4337).
Expiration date of individual notice: February 28, 1997
Local Public Document Room location: : Vespasian Warner Public
Library, 120 West Johnson Street, Clinton, Illinois 61727
Notice Of Issuance Of Amendments To Facility Operating Licenses And
Final Determination Of No Significant Hazards Consideration And
Opportunity For A Hearing (Exigent Public Announcement Or Emergency
Circumstances)
During the period since publication of the last biweekly notice,
the Commission has issued the following amendments. The Commission has
determined for each of these amendments that the application for the
amendment complies with the standards and requirements of the Atomic
Energy Act of 1954, as amended (the Act), and the Commission's rules
and regulations. The Commission has made appropriate findings as
required by the Act and the Commission's rules and regulations in 10
CFR Chapter I, which are set forth in the license amendment.
Because of exigent or emergency circumstances associated with the
date the amendment was needed, there was not time for the Commission to
publish, for public comment before issuance, its usual 30-day Notice of
Consideration of Issuance of Amendment, Proposed No Significant Hazards
Consideration Determination, and Opportunity for a Hearing.
For exigent circumstances, the Commission has either issued a
Federal Register notice providing opportunity for public comment or has
used local media to provide notice to the public in the area
surrounding a licensee's facility of the licensee's application and of
the Commission's proposed determination of no significant hazards
consideration. The Commission has provided a reasonable opportunity for
the public to comment, using its best efforts to make available to the
public means of communication for the public to respond quickly, and in
the case of telephone comments, the comments have been recorded or
transcribed as appropriate and the licensee has been informed of the
public comments.
In circumstances where failure to act in a timely way would have
resulted, for example, in derating or shutdown of a nuclear power plant
or in prevention of either resumption of operation or of increase in
power output up to the plant's licensed power level, the Commission may
not have had an opportunity to provide for public comment on its no
significant hazards consideration determination. In such case, the
license amendment has been issued without opportunity for comment. If
there has been some time for public comment but less than 30 days, the
Commission may provide an opportunity for public comment. If comments
have been requested, it is so stated. In either event, the State has
been consulted by telephone whenever possible.
Under its regulations, the Commission may issue and make an
amendment immediately effective, notwithstanding the pendency before it
of a request for a hearing from any person, in advance of the holding
and completion of any required hearing, where it has determined that no
significant hazards consideration is involved.
The Commission has applied the standards of 10 CFR 50.92 and has
made a final determination that the amendment involves no significant
hazards consideration. The basis for this determination is contained in
the documents related to this action. Accordingly, the amendments have
been issued and made effective as indicated.
Unless otherwise indicated, the Commission has determined that
these amendments satisfy the criteria for categorical exclusion in
accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b),
no environmental impact statement or environmental assessment need be
prepared for these amendments. If the Commission has prepared an
environmental assessment under the special circumstances provision in
10 CFR 51.12(b) and has made a determination based on that assessment,
it is so indicated.
For further details with respect to the action see (1) the
application for amendment, (2) the amendment to Facility Operating
License, and (3) the Commission's related letter, Safety Evaluation
and/or Environmental
[[Page 6586]]
Assessment, as indicated. All of these items are available for public
inspection at the Commission's Public Document Room, the Gelman
Building, 2120 L Street, NW., Washington, DC, and at the local public
document room for the particular facility involved.
The Commission is also offering an opportunity for a hearing with
respect to the issuance of the amendment. By March 14, 1997, the
licensee may file a request for a hearing with respect to issuance of
the amendment to the subject facility operating license and any person
whose interest may be affected by this proceeding and who wishes to
participate as a party in the proceeding must file a written request
for a hearing and a petition for leave to intervene. Requests for a
hearing and a petition for leave to intervene shall be filed in
accordance with the Commission's ``Rules of Practice for Domestic
Licensing Proceedings'' in 10 CFR Part 2. Interested persons should
consult a current copy of 10 CFR 2.714 which is available at the
Commission's Public Document Room, the Gelman Building, 2120 L Street,
NW., Washington, DC and at the local public document room for the
particular facility involved. If a request for a hearing or petition
for leave to intervene is filed by the above date, the Commission or an
Atomic Safety and Licensing Board, designated by the Commission or by
the Chairman of the Atomic Safety and Licensing Board Panel, will rule
on the request and/or petition; and the Secretary or the designated
Atomic Safety and Licensing Board will issue a notice of a hearing or
an appropriate order.
As required by 10 CFR 2.714, a petition for leave to intervene
shall set forth with particularity the interest of the petitioner in
the proceeding, and how that interest may be affected by the results of
the proceeding. The petition should specifically explain the reasons
why intervention should be permitted with particular reference to the
following factors: (1) the nature of the petitioner's right under the
Act to be made a party to the proceeding; (2) the nature and extent of
the petitioner's property, financial, or other interest in the
proceeding; and (3) the possible effect of any order which may be
entered in the proceeding on the petitioner's interest. The petition
should also identify the specific aspect(s) of the subject matter of
the proceeding as to which petitioner wishes to intervene. Any person
who has filed a petition for leave to intervene or who has been
admitted as a party may amend the petition without requesting leave of
the Board up to 15 days prior to the first prehearing conference
scheduled in the proceeding, but such an amended petition must satisfy
the specificity requirements described above.
Not later than 15 days prior to the first prehearing conference
scheduled in the proceeding, a petitioner shall file a supplement to
the petition to intervene which must include a list of the contentions
which are sought to be litigated in the matter. Each contention must
consist of a specific statement of the issue of law or fact to be
raised or controverted. In addition, the petitioner shall provide a
brief explanation of the bases of the contention and a concise
statement of the alleged facts or expert opinion which support the
contention and on which the petitioner intends to rely in proving the
contention at the hearing. The petitioner must also provide references
to those specific sources and documents of which the petitioner is
aware and on which the petitioner intends to rely to establish those
facts or expert opinion. Petitioner must provide sufficient information
to show that a genuine dispute exists with the applicant on a material
issue of law or fact. Contentions shall be limited to matters within
the scope of the amendment under consideration. The contention must be
one which, if proven, would entitle the petitioner to relief. A
petitioner who fails to file such a supplement which satisfies these
requirements with respect to at least one contention will not be
permitted to participate as a party.
Those permitted to intervene become parties to the proceeding,
subject to any limitations in the order granting leave to intervene,
and have the opportunity to participate fully in the conduct of the
hearing, including the opportunity to present evidence and cross-
examine witnesses. Since the Commission has made a final determination
that the amendment involves no significant hazards consideration, if a
hearing is requested, it will not stay the effectiveness of the
amendment. Any hearing held would take place while the amendment is in
effect.
A request for a hearing or a petition for leave to intervene must
be filed with the Secretary of the Commission, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-001, Attention: Docketing and Services
Branch, or may be delivered to the Commission's Public Document Room,
the Gelman Building, 2120 L Street, NW., Washington, DC, by the above
date. Where petitions are filed during the last 10 days of the notice
period, it is requested that the petitioner promptly so inform the
Commission by a toll-free telephone call to Western Union at 1-(800)
248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator
should be given Datagram Identification Number N1023 and the following
message addressed to (Project Director): petitioner's name and
telephone number, date petition was mailed, plant name, and publication
date and page number of this Federal Register notice. A copy of the
petition should also be sent to the Office of the General Counsel, U.S.
Nuclear Regulatory Commission, Washington, DC 20555-001, and to the
attorney for the licensee.
Nontimely filings of petitions for leave to intervene, amended
petitions, supplemental petitions and/or requests for a hearing will
not be entertained absent a determination by the Commission, the
presiding officer or the Atomic Safety and Licensing Board that the
petition and/or request should be granted based upon a balancing of the
factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden
Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
Date of application for amendments: January 13, 1997, as
resubmitted January 17, 1997, and supplemented January 22, 1997.
Brief description of amendments: The proposed amendments would:
evaluate the Unreviewed Safety Question (USQ) associated with the
operation of Dresden, Units 2 and 3, with the recently discovered error
in the head loss across the Emergency Core Cooling System (ECCS)
suction strainers; change the Technical Specification (TS) values by
lowering the allowable water temperature in the suppression chamber and
ultimate heat sink; change the basis of the TS to allow credit for two
psig of containment pressure to compensate for a slight increase in the
amount of Net Positive Suction Head (NPSH) deficiency during the first
10 minutes following a design basis accident (DBA); and add a license
condition to allow the licensee to change the Updated Final Safety
Analysis Report to reflect the use of two psig of containment pressure
to compensate for the deficiency in NPSH during the first 10 minutes
following a DBA.
Date of Issuance: January 28, 1997 Effective date: Immediately, to
be implemented within 30 days.
Amendment Nos.: 152/147
Facility Operating License Nos. DPR-19 and DPR-25. The amendments
revised the Technical Specifications and the Operating Licenses. Press
release issued requesting comments as to proposed no significant
hazards
[[Page 6587]]
consideration: Yes January 25, 1997 Joliet Herald News Comments
received: No. The Commission's related evaluation of the amendment,
finding of exigent circumstances, consultation with the State of
Illinois and determination of no significant hazards consideration are
contained in a Safety Evaluation dated January 28, 1997.
Attorney for licensee: Michael I. Miller, Esquire; Sidley and
Austin, One First National Plaza, Chicago, Illinois 60690
Local Public Document Room location: Morris Area Public Library
District, 604 Liberty Street, Morris, Illinois 60450.
NRC Project Director: Robert A. Capra
Dated at Rockville, Maryland, this 5th day of February, 1997.
For the Nuclear Regulatory Commission
Jack W. Roe,
Director, Division of Reactor Projects III/IV, Office of Nuclear
Reactor Regulation
[Doc. 97-3324 Filed 2-11-97; 8:45 am]
BILLING CODE 7590-01-F