X97-20212. Biweekly Notice  

  • [Federal Register Volume 62, Number 29 (Wednesday, February 12, 1997)]
    [Notices]
    [Pages 6566-6587]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X97-20212]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is
    
    [[Page 6567]]
    
    publishing this regular biweekly notice. Public Law 97-415 revised 
    section 189 of the Atomic Energy Act of 1954, as amended (the Act), to 
    require the Commission to publish notice of any amendments issued, or 
    proposed to be issued, under a new provision of section 189 of the Act. 
    This provision grants the Commission the authority to issue and make 
    immediately effective any amendment to an operating license upon a 
    determination by the Commission that such amendment involves no 
    significant hazards consideration, notwithstanding the pendency before 
    the Commission of a request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from January 17, 1997, through January 31, 1997. 
    The last biweekly notice was published on January 29, 1997 (62 FR 
    4341).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By March 14, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no
    
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    significant hazards consideration. The final determination will serve 
    to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: November 26, 1996
        Description of amendment request: The proposed amendment would 
    change the definition of ``Primary Containment Integrity,'' Note 6 on 
    Table 3.2.A, correct a typographical error on Table 3.2 D, correct 
    Table 3.2.F to reflect modifications to the plant and changes to Bases 
    sections 3/4.6G and 3/4.7.A. These changes are considered 
    administrative and have no effect on plant design, safety limit 
    settings or plant system operation.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        . The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed administrative changes involving typographical 
    errors, additions for clarity and consistency, and updating the 
    Bases do not affect plant design, safety limit settings, or plant 
    system operation and, therefore, do not modify or add any initiating 
    parameters that would significantly increase the probability or 
    consequences of any previously analyzed accident.
        The changes to instrument numbers and type do not change the 
    parameters being surveyed or the number of operable channels for 
    these parameters. These changes do not modify or add any initiating 
    parameters and do not affect plant design, safety limit settings, or 
    plant system operation. Therefore, these instrument changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        These proposed changes do not involve any potential initiating 
    events that would create any new or different kind of accident. 
    Therefore, the proposed changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        These changes do not affect any safety analysis assumptions, 
    system operation, structures, potential initiating events or safety 
    limits. Therefore, it is concluded that the proposed amendment does 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Patrick D. Milano, Acting
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: January 24, 1997
        Description of amendment request: The proposed amendment will 
    update the Safety Limit Minimum Critical Power Ratio (SLMCPR) in 
    Technical Specification (TS) 2.1.2 and the associated Bases section to 
    reflect the results of the latest cycle-specific calculation performed 
    for the Pilgrim Nuclear Power Station Operating Cycle 12. In addition, 
    the values provided in Note 5 of Table 3.2.C.1, which are based on the 
    SLMCPR values, have been revised as a result of the changes to the 
    SLMCPR value.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below: 11.The proposed technical specification changes do not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The derivation of the revised SLMCPR for Pilgrim for 
    incorporation into the TS, and its use to determine cycle-specific 
    thermal limits, have been performed using NRC approved methods. 
    Additionally, interim implementing procedures that incorporate 
    cycle-specific parameters have been used which result in a more 
    restrictive value for SLMCPR. These calculations do not change the 
    method of operating the plant and have no effect on the probability 
    of an accident initiating event or transient.
        The basis of the MCPR [minimum critical power ratio] Safety 
    Limit is to ensure no mechanistic fuel damage is calculated to occur 
    if the limit is not violated. The new SLMCPR preserves the existing 
    margin to transition boiling, and the probability of fuel damage is 
    not increased.
        The basis of the MCPR criteria that define a limiting rod 
    pattern is to ensure the SLMCPR is not violated in the event a 
    control rod is fully withdrawn from the core. The new MCPR criteria 
    that define a limiting rod pattern continue to ensure the SLMCPR is 
    not violated in the event a control rod is fully withdrawn from the 
    core. These new criteria do not change the method of operating the 
    plant and have no effect on the probability of an accident 
    initiating event or a transient.
    
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        Therefore, the proposed changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes result only from a revised method of 
    analysis for the Cycle 12 core reload. These changes do not involve 
    any new method for operating the facility and do not involve any 
    facility modifications. No new initiating events or transients 
    result from these changes. Therefore, the proposed TS changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety as defined in the TS bases will remain the 
    same. The new SLMCPR is calculated using NRC approved methods which 
    are in accordance with the current fuel design and licensing 
    criteria. Additionally, interim implementing procedures, which 
    incorporate cycle-specific parameters, have been used. The SLMCPR 
    remains high enough to ensure that greater than 99.9% of all fuel 
    rods in the core will avoid transition boiling if the limit is not 
    violated, thereby preserving the fuel cladding integrity.
        The new MCPR criteria that define a limiting rod pattern 
    continue to ensure the SLMCPR is not violated in the event a control 
    rod is fully withdrawn from the core.
        Therefore, the proposed TS changes do not involve a reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Patrick D. Milano, Acting
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: January 29, 1997
        Description of amendment request: The proposed change adds a new 
    entry 3.0.5 to the plant Technical Specifications (TS) to provide 
    specific guidance for returning equipment to service under 
    administrative control for the sole purpose of performing testing to 
    demonstrate operability.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change does not affect the operation or design of 
    the plant in any way. Operation of plant equipment under this change 
    will not differ in any way from its normal operational mode. The 
    normal operation of plant equipment is not a precursor to any 
    accident. The purpose of tests performed using this change are to 
    demonstrate that required automatic actions are carried out. 
    Equipment will be operated under administrative control for only a 
    short period of time. Personnel will be immediately available to 
    take appropriate manual action if it should be required. Therefore 
    operation of equipment under this change is not expected to increase 
    the probability or consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed testing allowance does not involve any physical 
    alterations or additions to plant equipment or alter the manner in 
    which any safety-related system performs its function. Therefore, 
    the proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3.
        The proposed amendment does not involve a signifcant reduction in 
    the margin of safety.
        Equipment will be operated under administrative control for only 
    a short period of time. Personnel will be immediately available to 
    take appropriate manual action if it should be required. The purpose 
    of the testing is to restore required equipment to an OPERABLE state 
    which increases the automatic protection available and reduces the 
    reliance on the compensatory measures provided by ACTION statements. 
    Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Mark Reinhart, Acting
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: October 24, 1996
        Description of amendment request: The proposed amendment to the 
    Perry Nuclear Power Plant Technical Specifications revises those 
    specifications associated with the Minimum Critical Power Ratio (MCPR) 
    Reactor Core Safety Limit. The revision would increase the MCPR Safety 
    Limit values to make them more conservative.
        Basis for proposed no significant hazards determination: The NRC 
    staff provides its analysis of the issue of no significant hazards 
    consideration below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        There is no change to any plant equipment, and increasing the 
    MCPR Safety Limit is more conservative. Therefore, the proposed 
    change does not significantly increase the probability or 
    consequences of any accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There are no physical changes to the plant, and increasing the MCPR 
    Safety Limit is more conservative. Therefore, the proposed changes do 
    not create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed MCPR Safety Limit values are more conservative, and 
    were calculated using NRC approved methods. Therefore, the proposed 
    change does not involve a significant reduction in a margin of safety.
        The staff has reviewed the amendment request and the licensee's no 
    significant hazards consideration determination. Based on the review 
    and the above discussions, the staff proposes to determine that the 
    proposed changes do not involve a significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
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    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: August 19, 1996
        Description of amendment request: The proposed amendments revise 
    the steam generator (SG) repair criteria in the Byron, Unit 1, and 
    Braidwood, Unit 1, Technical Specifications (TS). These revisions, if 
    approved, would continue the use of the voltage-based SG tube repair 
    criteria added by Amendment No. 77, dated November 9, 1995, to the 
    Byron 1 TSs and by Amendment No. 69, dated November 9, 1995, to the 
    Braidwood 1 TSs. The subject voltage-based repair criteria are 
    applicable only for a specific form of SG tube degradation identified 
    as outer diameter stress corrosion cracking (ODSCC), which is confined 
    entirely within the thickness of the SG tube support plates (TSPs). 
    Specifically, the pending amendments for both units would continue for 
    one more operating cycle, the present use of a lower voltage repair 
    limit of 3.0 volts on the hot leg side of the SGs using the Locked-Tube 
    model. The cold leg side of the SGs and certain hot leg side tube/TSP 
    intersections (e.g., dented SG tube intersections) would continue to be 
    repaired using the Free-Span model. The proposed amendments are needed 
    because the applicability of the revised voltage-based SG tube repair 
    criteria for ODSCC which were added in the prior amendments cited 
    above, was limited to only one full operating cycle for Braidwood 1 
    ending in spring 1997 and for the operating cycle ending in late 1997 
    for Byron 1.
        Additionally, the inspection and reporting requirements added to 
    the Byron 1 and Braidwood 1 TSs by the prior amendments cited above, 
    would also be continued for one more operating cycle for both units. 
    The maximum permissible value of the iodine-131 concentration in the 
    primary coolant in both the Byron 1 and Braidwood 1 TSs remains 
    unchanged at 0.35 microcuries per gram of coolant. Finally, the Bases 
    sections in the Byron 1 and Braidwood 1 TSs are proposed to be revised 
    to introduce the terminology associated with the Locked-Tube SG tube 
    model and that of the Free-Span model.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This amendment request proposes to renew the SG tube plugging/
    repair criteria previously approved by the NRC in Amendments 69 and 
    77 to Braidwood and Byron Technical Specifications, respectively.
        The previously evaluated applicable accidents are steam 
    generator tube burst and Main Steam Line Break (MSLB). The 
    postulated MSLB outside of containment but upstream of the Main 
    Steam Isolation Valve (MSIV) represents the most limiting 
    radiological condition relative to the IPC. The potential impact on 
    public health and safety as a result of renewing the SG tube interim 
    plugging criteria contained in the current Braidwood and Byron 
    Technical Specifications is very low as discussed below. Tube burst 
    due to predominantly axially oriented ODSCC at the TSP intersections 
    is precluded during normal operating plant conditions since the tube 
    support plates are adjacent to the degraded regions of the tube in 
    the tube-to-tube support plate crevices.
        During accident conditions, i.e., MSLB, the tubes and TSP may 
    move relative to each other. This can expose the crack length 
    portion to free-span conditions. Testing has shown that the burst 
    pressure correlates to the crack length that is exposed to the free-
    span, regardless of the length that is still contained within the 
    TSP bounds.
        Therefore, a more appropriate methodology has been established 
    for addressing leakage and burst considerations. This methodology is 
    based on limiting potential TSP displacements (Locked-Tube Model 
    Intersections) during postulated MSLB events, thus reducing the 
    free-span exposed crack length to minimal levels. The tube expansion 
    process employed in conjunction with this tube plugging criteria is 
    designed to provide postulated TSP displacements that result in 
    negligible tube burst probabilities due to the minimal free-span 
    exposed crack lengths. The tube expansions were performed during the 
    first outage that the 3.0 volt IPC was applied (Braidwood refuel 
    outage A1R05 -Fall 1995, and Byron midcycle outage B1P02 - Fall 
    1995). These expansions will be inspected in accordance with an eddy 
    current inspection probe that is sensitive to axial and 
    circumferential indications. This program will ensure the integrity 
    of the expansions for the additional cycle of operation. It has been 
    demonstrated that axial indications in the expansion region will not 
    result in a reduction of the load carrying capability of the 
    expanded tubes.
        Thermal hydraulic modeling was used to determine TSP loading 
    during MSLB conditions. A safety factor was conservatively applied 
    to these loads to envelope the collective uncertainties in the 
    analyses. Various operating conditions were evaluated and the most 
    limiting operating condition was used in the analyses. Additional 
    models were used to verify the thermal hydraulic results.
        Assessment of the tube burst probability for the Locked-Tube 
    Model Intersections was based on a conservative assumption that all 
    hot-leg TSP intersections (32,046) contained through wall cracks 
    equal to the postulated TSP displacement and that the crack lengths 
    were located within the boundaries of the TSP. Alternatively, it was 
    assumed that all hot-leg TSP intersections contained through wall 
    cracks with lengths equal to the thickness of the TSP. The 
    postulated TSP motion was conservatively assumed to be uniform and 
    equal to the maximum displacement calculated.
        The total burst probability for all 32,046 through wall 
    indications, given a uniform MSLB TSP displacement of 0.31 inches, 
    was calculated to be 1x10-5. This is a factor of 1000 less than 
    the GL 95-05 burst probability limit of 1x10-2. Therefore, the 
    functional design criteria for tube expansion was to limit the TSP 
    motion to 0.31'' or less. However, the design goal for tube 
    expansion limits the TSP MSLB motion to less than 0.1''. This design 
    goal results in a total tube burst probability of 1x10-10 for 
    all 32,046 postulated through wall indications. Additional tubes 
    were expanded to provide redundancy for the required expansions.
        The structural limit for the Locked-Tube Model Intersection SG 
    tube repair criteria was based on axial tensile loading requirements 
    to preclude axial tensile severing of the tube. Axially oriented 
    ODSCC does not significantly impact the axial tensile loading of the 
    tube. Based on the current voltage distributions and growth rates, 
    Monte Carlo projections were performed for Braidwood Unit 1 and 
    Byron Unit 1 for the additional cycle of operation that this 
    proposed amendment is requesting. The End of Cycle (EOC) voltage 
    projections for Braidwood Unit 1 Cycle 7 predict that the maximum 
    voltage to be seen will be less than 10.5 volts. The number of 
    indications predicted greater than ten volts at the end of Cycle 7 
    for Braidwood Unit 1 is 0.3. The EOC voltage projections for Byron 
    Unit 1 Cycle 9 predict that the maximum voltage to be seen will be 
    less than 13.5 volts. The number of indications predicted greater 
    than ten volts at the end of Cycle 9 for Byron Unit 1 is 4.59.
        Using a tensile rupture probability for a ten volt indication of 
    3x10-6, the probability of tensile rupture from the predicted 
    0.3 indications at Braidwood is 1-(1-3x10-6)0.3 = 
    9.0x10-7. The probability of tensile rupture from the predicted 
    4.59 indications at Byron is 1-(1-3x10-6)4.59 = 
    1.38x10-5. Both of these probabilities result in a negligible 
    contribution to the total burst probability when compared to the 
    1x10-2 GL 95-05 limit.
        Cellular corrosion is a more limiting mode of degradation at the 
    TSPs with respect to affecting the tube structural limit. Tensile 
    tests that measure the force required to sever a tube with cellular 
    corrosion and uncorroded cross sectional areas are used to establish 
    the lower bound structural limit. Based upon these tests, a lower 
    bound 95% confidence level structural voltage limit of 37 volts was 
    established for cellular corrosion. This limit meets the Regulatory 
    Guide (RG) 1.121, ``Basis for Plugging Steam Generator Tubes,'' 
    structural requirements based upon the normal operating pressure 
    differential with a safety factor of 3.0 applied. Due to the limited 
    database supporting this value, the
    
    [[Page 6571]]
    
    structural limit was conservatively reduced to 20 volts. Accounting 
    for voltage growth and Non-Destructive Examination (NDE) 
    uncertainty, the full IPC upper limit exceeds ten volts. However, 
    for added conservatism a single voltage repair limit of 3.0 volts 
    for the Locked-Tube Model Intersection indications is specified in 
    the current plugging/repair criteria. All indications at the Locked 
    Tube Model Intersections with bobbin coil probe voltages greater 
    than 3.0 volts will be plugged or repaired.
        The free-span tube burst probability must be calculated for the 
    indications at the Free-Span Model Intersections. The total burst 
    probability must be within the requirements of GL 95-05. The free-
    span structural voltage limit is calculated using correlations from 
    the database described in GL 95-05, with the inclusion of the recent 
    Byron, Braidwood, and South Texas tube pull results. The structural 
    limit for the Free-Span Model Intersections is 4.745 volts. The 
    lower voltage repair limit for the indications at the Free-Span 
    Model Intersections continues to be 1.0 volt. The upper voltage 
    repair limit for the indications at the Free-Span Model 
    Intersections will be calculated in accordance with GL 95-05.
        Since IPC will not be applied to indications at the Flow 
    Distribution Baffle (FDB), no leakage or burst analyses are required 
    for these indications.
        Per GL 95-05, MSLB leak rate and tube burst probability analyses 
    are required to be performed prior to returning the unit to power. 
    The results of these analyses are to be included in a report to the 
    NRC within 90 days of restart. If allowable limits on leak rates and 
    burst probability are exceeded, the results are to be reported to 
    the NRC and a safety assessment of the significance of the results 
    is to be performed prior to returning the SGs to service.
        A site specific calculation has determined the site allowable 
    leakage limit for Braidwood and Byron. These limits use the 
    recommended Dose Equivalent Iodine-131 transient spiking values 
    consistent with NUREG-0800, ``Standard Review Plan'' and ensure site 
    boundary doses are within a small fraction of the 10 CFR 100 
    requirements.
        The projected leakage rate calculation methodology described in 
    WCAP-14046, ``Braidwood Unit 1 Technical Support for Cycle 5 Steam 
    Generator Interim Plugging Criteria,'' and WCAP-14277, ``SLB Leak 
    Rate and Tube Burst Probability Analysis Methods for ODSCC at TSP 
    Intersections,'' will be used to calculate the EOC leakage. This 
    method includes a Probability of Detection (POD) value of 0.6 for 
    all voltage amplitude ranges and uses the accepted leak rate versus 
    bobbin voltage correlation methodology (full Monte Carlo) for 
    calculating the leak rate, as described in GL 95-05. The database 
    used for the leak and burst correlations is consistent with that 
    described in GL 95-05 with the inclusion of the Byron Unit 1, 
    Braidwood Unit 1, and South Texas tube pull results. The EOC voltage 
    distribution is developed from the POD adjusted beginning-of-cycle 
    (BOC) voltage distributions and uses Monte Carlo techniques to 
    account for variances in growth and NDE uncertainty.
        The Electric Power Research Institute (EPRI) leak rate 
    correlation has been used. This correlation is based on free-span 
    indications that have burst pressures above the MSLB pressure 
    differential. There is a low but finite probability that indications 
    may burst at a pressure less than MSLB pressure. With limited TSP 
    motion for the Locked-Tube Model Intersections, the tube is 
    constrained by the TSP and tube burst is precluded. However, the 
    flanks of the crack may open up to contact the Inside Diameter (ID) 
    of the TSP hole and result in a primary-to-secondary leak rate 
    potentially exceeding that obtained from the EPRI correlation. This 
    phenomenon is known as an Indication Restricted from Burst (IRB) 
    condition.
        ComEd has performed laboratory testing to determine the bounding 
    leak rate obtainable in an IRB condition (6.0 gallons per minute). 
    The bounding leak rate value was then applied to a leak rate 
    calculation methodology that accounts for the MSLB leak rate 
    contribution from IRB indications to the total leak rate calculated 
    as described above. Results indicate that the IRB contribution to 
    the total leak rate value is negligible. However, ComEd will 
    conservatively add a leakage contribution due to IRBs in addition to 
    the leakage calculated in accordance with GL 95-05. When this is 
    done, the dose at the site boundary resulting from the predicted 
    leakage will be a small fraction (less than 10%) of the 10 CFR 100 
    limits.
        Modification of the Braidwood and Byron TS to clarify 
    application of the proposed tube plugging/repair criteria is purely 
    administrative and will not have any effect on the probability or 
    consequences of an accident previously evaluated.
        Operating experience over the last cycle with this plugging 
    criteria applied has not revealed any unpredicted or unusual 
    effects.
        For these reasons, renewal of the current Braidwood and Byron 
    tube plugging criteria does not adversely affect SG tube integrity 
    and results in acceptable dose consequences. By effectively 
    eliminating tube burst at the Locked-Tube Model TSP intersections, 
    the likelihood of a tube rupture is substantially reduced and the 
    probability of occurrence of an accident previously evaluated is 
    reduced.
        This conclusion is not affected by foreign or domestic plant SG 
    experiences (NRC Information Notice 96-09 and its supplement). As 
    the following evaluation shows, these experiences are not relevant 
    to Braidwood or Byron.
        A foreign unit detected eddy current signal distortions in one 
    area of the top TSP during a 1995 inspection. The steam generators 
    had been chemically cleaned in 1992. Visual inspection showed that a 
    small section of the top TSP had broken free and was resting next to 
    the steam generator tube bundle wrapper. The support plate showed 
    indications of metal loss.
        The chemical cleaning process used by the foreign unit was 
    developed by the utility and differs significantly from the modified 
    EPRI/SGOG process performed at Byron Unit 1 in 1994. The foreign 
    chemical cleaning process, coupled with the specific application of 
    the process, resulted in TSP corrosion of up to 250 mils compared to 
    a maximum of 2.16 mils (11 mils maximum allowed) measured at Byron. 
    During the Byron eddy current inspection performed after the 
    chemical cleaning, no distortion of the tube support plate signals 
    was reported. Therefore, these differences in cleaning processes 
    imply that this foreign experience is irrelevant to the effects of 
    the chemical cleaning process on the TSPs at Byron. Chemical 
    cleaning of the SGs has not occurred at Braidwood.
        A number of units have experienced TSP cracking associated with 
    severe tube denting due to TSP corrosion at the tube-to-TSP crevice. 
    WCAP-14273, Section 12.4, shows that a diametral reduction of a SG 
    tube of 0.065 inches is required to develop stress levels above 
    yield in the TSP ligaments at dented intersections. The bobbin 
    voltage range associated with a one mil radial dent is twenty to 
    twenty-five volts.
        Although Braidwood Unit 1 and Byron Unit 1 have not seen 
    corrosion induced denting, a 0.610 inch diameter bobbin coil probe 
    will be used as a go/no-go gauge to assess dents at the Locked-Tube 
    Model Intersections, if they occur in the future. If a tube has a 
    dent at a Locked-Tube Model TSP intersection that fails to pass the 
    go/no-go test probe, IPC will not be applied to that intersection. 
    In addition, if the dent is determined to be corrosion induced, the 
    Free-Span Model repair criteria will be applied to the intersections 
    adjacent to the dented intersection. IPC repair limits will not be 
    applied to tubes with dents greater than 5.0 volts since dent 
    signals of this magnitude could mask a 1.0 volt ODSCC signal. Tube 
    intersections with corrosion induced dents greater than 5.0 volts 
    and the intersections adjacent to such an intersection were not 
    selected for tube expansion to preclude adverse effects of the 
    failure of such a tube on limiting TSP displacement. If corrosion 
    induced denting, either greater than 5.0 volts or such that the tube 
    is unable to pass a 0.610 inch diameter bobbin coil probe, are 
    detected at an intersection adjacent to an expanded intersection, 
    the dented intersection will be inspected by an EPRI developed 
    technique to determine if the TSP is cracked. If a crack-like 
    indication is identified in a TSP, a plus point inspection will be 
    conducted per the EPRI TSP program. If the plus point inspection 
    verifies the existence of a crack-like indication, the effect of 
    that indication on TSP displacement will be evaluated. If this 
    evaluation shows that TSP displacement would be greater than 0.1 
    inches during a MSLB event, the effected area will either be 
    mechanically corrected or the Free-Span Model criteria will be 
    applied to the affected area. Based on the information presented 
    above, the SG tube denting experience at other plants is not 
    relevant to Braidwood or Byron.
        A foreign utility's SGs have experienced cracking at the top 
    TSP. The cause of the cracking appears to be the configuration of 
    the single anti-rotation device, connected between the SG shell and 
    wrapper, and the wrapper internals. The single anti-rotation device 
    carries the full load associated with the wrapper to shell motion. 
    This rotational load is believed to be transferred to the TSP via 
    the wrapper internals. The Byron/Braidwood Unit 1 SG design (D-4) 
    uses three anti-rotation devices to spread the rotational load. The 
    D-4 wrapper internals are configured such that this load is not 
    directly transmitted to the TSP.
    
    [[Page 6572]]
    
        No top TSP cracking has been detected at Braidwood Unit 1 or 
    Byron Unit 1 and very few (<1%) of="" the="" odscc="" indications="" in="" the="" sg="" tubes="" at="" braidwood="" and="" byron,="" to="" date,="" have="" been="" at="" the="" top="" tsp="" elevation.="" nevertheless,="" an="" analysis="" was="" performed="" to="" assess="" the="" impact="" of="" cracking="" of="" the="" top="" tsp.="" the="" results="" show="" an="" increase="" in="" the="" deflection="" of="" the="" top="" tsp="" for="" a="" very="" limited="" number="" of="" tubes="" to="" greater="" than="" the="" 0.10''="" limit="" used="" in="" the="" 3.0="" volt="" ipc="" analysis.="" the="" deflections="" of="" the="" lower="" support="" plates="" also="" increased,="" but="" remain="" within="" the="" 0.10''="" limit.="" thus,="" a="" large="" majority="" of="" the="" locked-tube="" model="" indications="" continue="" to="" be="" bounded="" by="" the="" existing="" analysis="" even="" with="" a="" cracked="" top="" tsp.="" the="" locked-tube="" model="" repair="" criteria="" will="" not="" be="" applied="" to="" any="" sg="" tube="" odscc="" indication="" where="" the="" tsp="" has="" been="" shown="" to="" be="" displaced="" by="" more="" than="" 0.1="" inches="" during="" accident="" conditions.="" in="" response="" to="" these="" experiences="" at="" foreign="" and="" domestic="" utilities,="" comed="" developed="" an="" inspection="" plan="" for="" the="" sg="" internals="" to="" identify="" if="" indications="" detrimental="" to="" the="" load="" path="" components="" existed.="" this="" inspection="" plan="" was="" carried="" out="" at="" braidwood="" during="" refueling="" outage="" a1r05="" (fall="" 1995)="" and="" at="" byron="" during="" the="" midcycle="" outage="" b1p02="" (fall="" 1995)="" and="" refuel="" outage="" b1r07="" (spring="" 1996).="" these="" inspections="" revealed="" no="" degradation="" of="" the="" sg="" load="" path="" components="" necessary="" to="" support="" implementation="" of="" the="" 3.0="" volt="" ipc.="" inspections="" will="" be="" performed="" during="" the="" upcoming="" refuel="" outages="" at="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" to="" further="" ensure="" the="" integrity="" of="" the="" sg="" load="" path="" components="" necessary="" to="" support="" implementation="" of="" the="" 3.0="" volt="" ipc.="" a="" domestic="" utility="" reported="" several="" distorted="" tsp="" signals="" over="" the="" past="" three="" refueling="" outages'="" sg="" tube="" inspections.="" it="" was="" determined="" that="" these="" signals="" were="" associated="" with="" the="" tsp="" geometry="" in="" an="" area="" where="" an="" access="" cover="" is="" welded="" to="" the="" tsp.="" these="" signal="" distortions="" are="" not="" attributed="" to="" tsp="" cracking="" or="" degradation.="" since="" the="" distorted="" signals="" were="" due="" to="" tsp="" geometry="" which="" did="" not="" indicate="" or="" result="" in="" a="" defect="" of="" the="" tsp,="" there="" is="" no="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" due="" to="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" steam="" generator="" tsp="" geometries="" which="" may="" result="" in="" distorted="" eddy="" current="" signals.="" one="" foreign="" unit="" observed="" a="" dislocation="" of="" the="" tube="" bundle="" wrapper="" when="" they="" were="" unable="" to="" pass="" sludge="" lancing="" equipment="" through="" a="" hand="" hole="" in="" the="" wrapper.="" the="" dislocation="" appears="" to="" be="" a="" result="" of="" improper="" attachment="" of="" the="" wrapper="" to="" the="" support="" structure.="" sg="" sludge="" lance="" operations="" have="" been="" successfully="" performed="" at="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" which="" indicates="" that="" no="" problem="" with="" the="" wrapper="" attachment="" exists.="" the="" foreign="" unit's="" wrapper="" support="" design="" is="" significantly="" different="" than="" that="" used="" on="" braidwood="" unit="" 1="" and="" byron="" unit="" 1.="" therefore,="" a="" similar="" wrapper="" dislocation="" will="" not="" occur="" and="" the="" foreign="" experience="" is="" not="" applicable="" to="" braidwood="" or="" byron.="" an="" inspection="" was="" conducted="" during="" the="" last="" braidwood="" unit="" 1="" and="" byron="" unit="" 1="" refueling="" outages="" which="" verified="" this="" conclusion.="" comed="" will="" continue="" to="" apply="" a="" maximum="" primary-to-secondary="" leakage="" limit="" of="" 150="" gallons="" per="" day="" (gpd)="" through="" any="" one="" sg="" at="" braidwood="" and="" byron="" to="" help="" preclude="" the="" potential="" for="" excessive="" leakage="" during="" all="" plant="" conditions.="" the="" rg="" 1.121="" criterion="" for="" establishing="" operational="" leakage="" limits="" that="" require="" plant="" shutdown="" are="" based="" on="" detecting="" a="" free-span="" crack="" prior="" to="" it="" resulting="" in="" primary-to-secondary="" operational="" leakage="" which="" could="" potentially="" develop="" into="" a="" tube="" rupture="" during="" faulted="" plant="" conditions.="" the="" 150="" gpd="" limit="" provides="" for="" leakage="" detection="" and="" plant="" shutdown="" in="" the="" event="" of="" an="" unexpected="" single="" crack="" leak="" associated="" with="" the="" longest="" permissible="" free-span="" crack="" length.="" therefore,="" the="" proposed="" amendment="" does="" not="" result="" in="" any="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" within="" the="" braidwood="" and="" byron="" updated="" final="" safety="" analysis="" report="" (ufsar).="" 2.="" the="" proposed="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" this="" amendment="" request="" proposes="" to="" renew="" the="" sg="" tube="" plugging/="" repair="" criteria="" previously="" approved="" by="" the="" nrc="" in="" amendments="" 69="" and="" 77="" to="" braidwood="" and="" byron="" technical="" specifications,="" respectively.="" renewal="" of="" the="" proposed="" steam="" generator="" tube="" plugging="" criteria="" with="" tube="" expansion="" does="" not="" introduce="" any="" significant="" changes="" to="" the="" plant="" design="" basis.="" use="" of="" the="" criteria="" does="" not="" provide="" a="" mechanism="" which="" could="" result="" in="" an="" accident="" outside="" of="" the="" region="" of="" the="" tube="" support="" plate="" elevations="" as="" odscc="" does="" not="" extend="" beyond="" the="" thickness="" of="" the="" tube="" support="" plates="" and="" ipc="" is="" not="" allowed="" to="" be="" applied="" to="" indications="" that="" extend="" beyond="" the="" thickness="" of="" the="" tube="" support="" plate.="" neither="" a="" single="" nor="" multiple="" tube="" rupture="" event="" would="" be="" expected="" in="" a="" sg="" in="" which="" the="" plugging="" criteria="" has="" been="" applied.="" the="" tube="" burst="" assessment="" involves="" a="" monte="" carlo="" simulation="" of="" the="" site="" specific="" voltage="" distribution="" to="" generate="" a="" total="" burst="" probability="" that="" includes="" the="" summation="" of="" the="" probabilities="" of="" one="" tube="" bursting,="" two="" tubes="" bursting,="" etc.="" for="" the="" locked-tube="" model="" tsp="" intersections,="" the="" maximum="" total="" probability="" of="" burst,="" by="" design,="" is="" estimated="" to="" be="">-10 with all tube expansions 
    functional. The burst probability for the Free-Span Model TSP 
    intersections will be dependent on the number and size of 
    indications at these applicable intersections. The total burst 
    probability will be within the limit specified in GL 95-05.
        Accounting for the unlikely event of a failure of the expanded 
    tubes, a sufficient number of redundant expansions exist to ensure 
    that the burst probability remains below 1x10-5. This includes 
    the conservative assumption that all 32,046 hot-leg TSP 
    intersections contain through wall indications. This level of burst 
    probability is considered to be negligible when compared to the GL 
    95-05 limit of 1x10-2.
        In addressing the combined effects of a Loss Of Coolant Accident 
    (LOCA) during a Safe Shutdown Earthquake (SSE) on the SG as required 
    by General Design Criteria (GDC) 2, it has been determined that tube 
    collapse may occur in the steam generators at some plants. The tube 
    support plates may become deformed as a result of lateral loads at 
    the wedge supports located at the periphery of the plate due to the 
    combined effects of the LOCA rarefaction wave and SSE loadings. The 
    resulting pressure differential on the deformed tubes may cause some 
    of the tubes to collapse. There are two issues associated with SG 
    tube collapse. First, the collapse of SG tubing reduces the Reactor 
    Coolant System (RCS) flow area through the tubes. The reduction in 
    flow area increases the resistance to flow of steam from the core 
    during a LOCA which, in turn, may potentially increase the Peak Clad 
    Temperature (PCT). Second, there is a potential that partial through 
    wall cracks in the SG tubes could progress to through wall cracks 
    during tube deformation or collapse. The tubes subject to collapse 
    have been identified via a plant specific analysis and are excluded 
    from application of any voltage-based criteria. This analysis is 
    included in revision 3 to WCAP-14046 which was submitted to the NRC 
    June 19, 1995.
        Modification of the Braidwood and Byron Technical Specifications 
    to clarify application of the proposed tube plugging/repair criteria 
    is purely administrative and will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Operating experience over the last cycle with this plugging 
    criteria applied has not revealed any unpredicted or unusual 
    effects.
        SG tube integrity will continue to be maintained following 
    renewal of the 3.0 volt IPC voltage repair limit through inservice 
    inspection, tube repair and primary-to-secondary leakage monitoring. 
    By effectively eliminating tube burst at the Locked-Tube Model TSP 
    Intersections, the potential for multiple tube ruptures is 
    essentially eliminated.
        ComEd has evaluated industry experiences with TSP degradation, 
    eddy current signal distortions, and component misalignment. Eddy 
    current signal distortions due to TSP geometry are not indicative of 
    TSP degradation and do not result in any kind of new or different 
    accident.
        The component misalignment experienced by one unit is not 
    applicable to Braidwood Unit 1 or Byron Unit 1 and, thus, will not 
    result in any kind of new or different accident. Specific 
    limitations, as discussed in response to Question 1, will be applied 
    to indications at the Locked-Tube Model Intersections which contain 
    dents. These limitations ensure that the integrity of the SG tubes 
    is maintained consistent with the current analyses should tube 
    denting or TSP cracking occur.
        Therefore, renewal of the current tube plugging/repair criteria 
    at Braidwood Unit 1 and Byron Unit 1 will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The use of the voltage-based, bobbin coil, tube support plate 
    plugging criteria with tube expansion at Braidwood Unit 1 and Byron 
    Unit 1 is demonstrated to maintain SG tube integrity commensurate 
    with the criteria of RG 1.121. RG 1.121 describes a method
    
    [[Page 6573]]
    
    acceptable to the NRC staff for meeting GDC 14, 15, 31, and 32 by 
    reducing the probability or the consequences of steam generator tube 
    rupture.
        Reducing the probability or the consequences of steam generator 
    tube rupture is accomplished by determining an eddy current 
    inspection voltage value which represents a limit for leaving an 
    axial, crack-like indication at an in service SG tube TSP 
    intersection. Tubes with ODSCC voltage indications beyond this 
    limiting value must be removed from service by plugging or repaired 
    by sleeving. Implementation of a 3.0 volt IPC voltage repair limit 
    for the Locked-Tube Model Intersections has been evaluated and shown 
    not to present a credible potential for a steam generator tube 
    rupture event during normal or faulted plant conditions, even with 
    worst case assumptions. The total tube burst probability will 
    include a contribution from the indications at the Locked-Tube Model 
    Intersections and from indications at the Free-Span Model 
    Intersections. The projected EOC voltage distribution of crack-like 
    indications at the TSP elevations will be confirmed to result in 
    acceptable primary-to-secondary leakage during all plant conditions 
    such that radiological consequences are not adversely impacted.
        Addressing RG 1.83 considerations, implementation of the 
    increased Locked-Tube Model Intersection bobbin coil voltage-based 
    repair criteria is supplemented by enhanced eddy current inspection 
    guidelines to provide consistency in voltage normalization and a 
    100% eddy current inspection sample size at the affected TSP 
    elevations.
        For the leak and burst assessments, the population of 
    indications in the EOC voltage distribution is dependent on the POD 
    function. The purpose of the POD function is to account for new 
    indications that may develop over the cycle, and to account for 
    indications not identified by the data analyst. In implementing this 
    proposed IPC renewal, ComEd will continue to use the conservative GL 
    95-05 POD value of 0.6 for all voltage amplitude ranges.
        Modification of the Braidwood and Byron Technical Specifications 
    to clarify application of the proposed tube plugging/repair criteria 
    is purely administrative and will not reduce any safety margins.
        Operating experience over the last cycle with this plugging 
    criteria applied has not revealed any unpredicted or unusual 
    effects.
        Implementation of the TSP elevation repair limits will decrease 
    the number of tubes which must be repaired. Installation of steam 
    generator tube plugs or sleeves reduces the RCS flow margin. Thus, 
    implementation of the IPC will maintain the margin of flow that 
    would otherwise be reduced in the event of increased tube plugging 
    or sleeving.
        As discussed previously, ComEd has evaluated industry 
    experiences with TSP degradation, eddy current signal distortions, 
    and component misalignment. Eddy current signal distortions at tube 
    support plates will be evaluated to attempt to determine the cause 
    of the distortion. A signal distortion alone will not result in 
    reduction in the margin of safety. The foreign unit that experienced 
    the component misalignment was of a significantly different design 
    than the Braidwood Unit 1 and Byron Unit 1 steam generators. 
    Analysis of the design differences shows that component misalignment 
    of that type is not applicable to Braidwood Unit 1 or Byron Unit 1 
    and, thus, will not result in a reduction in the margin of safety. 
    An inspection was conducted during the last Braidwood Unit 1 and 
    Byron Unit 1 refueling outages which verified this conclusion.
        Specific limitations, as discussed previously, will be applied 
    to indications at the Locked-Tube Model Intersections which contain 
    dents. These limitations conservatively treat indications as free-
    span to ensure that the integrity of the SG tubes is maintained 
    consistent with current analyses should tube denting or TSP cracking 
    occur. Application of the 3.0 volt Locked-Tube Model Intersection 
    IPC and the 1.0 volt Free-Span Model Intersection IPC at Braidwood 
    Unit 1 and Byron Unit 1, with the limitations specified, will not 
    result in a reduction in a margin of safety.
        Thus, the implementation of this amendment does not result in a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendment request: January 6, 1997
        Description of amendment request: The proposed amendment would 
    clarify and maintain consistency between the operability requirements 
    for protective instrumentation and associated automatic bypass 
    features.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
    1) Involve a significant increase in the probability or consequences of 
    an accident previously evaluated because of the following:
        The proposed changes are administrative in nature and do not 
    affect the probability or consequences of any previously evaluated 
    accidents for Dresden or Quad Cities Stations. The proposed 
    amendment is consistent with the current safety analyses and 
    represents sufficient requirements for the continued assurance and 
    reliability of the RPS and Rod Block Instrumentation equipment, 
    which is assumed to operate in the safety analysis, or provides 
    continued assurance that specified parameters associated with RPS 
    and Rod Block Instrumentation remain within their acceptance limits. 
    Therefore, these changes will not affect the probability or 
    consequences of a previously evaluated accident.
        The RPS and Rod Block Instrumentation related to this proposed 
    amendment is not assumed in any safety analysis to initiate any 
    accident sequence for Dresden or Quad Cities Stations; therefore, 
    the probability of any accident previously evaluated is not affected 
    by the proposed amendment.
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        The proposed changes are administrative in nature and serve to 
    maintain consistent and clear requirements for operability as 
    specified in the Technical Specifications for the Limiting 
    Conditions for Operation and Surveillance Requirements for the RPS 
    and Rod Block Instrumentation. No new modes of operation or changes 
    to any plant equipment are proposed by the proposed amendment 
    request. The associated systems related to this proposed amendment 
    are not assumed in any safety analysis to initiate any accident 
    sequence for Dresden or Quad Cities. The proposed changes maintain 
    the present level of operability; and therefore, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident than any previously evaluated.
        3) Involve a significant reduction in the margin of safety 
    because:
        The proposed changes are administrative in nature and do not 
    affect existing plant safety margins or the reliability of the 
    equipment assumed to operate in the safety analysis. The proposed 
    changes have been evaluated and found to be acceptable for use at 
    Dresden and at Quad Cities based on RPS and Rod Block 
    Instrumentation system design, safety analysis requirements and 
    operational performance. Since the proposed changes are 
    administrative in nature and maintain necessary levels of the RPS 
    and Rod Block reliability, the proposed changes do not involve a 
    reduction in the margin of safety.
        The proposed amendment for Dresden and Quad Cities Stations will 
    not reduce the availability of the RPS and Rod Block Instrumentation 
    System which is required to mitigate accident conditions; therefore, 
    the proposed changes do not involve a reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this
    
    [[Page 6574]]
    
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: October 22, 1996
        Description of amendment request: The proposed amendments would 
    allow continued plant operation at elevated Containment Lower 
    Compartment temperatures between 125 deg. and 135 deg. F for a period 
    not to exceed 72 cumulative hours.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. Does the proposed amendment involve a significant increase in 
    the probability or consequences of any accident previously evaluated 
    in the UFSAR [Updated Final Safety Analysis Report]?
        The increase in maximum Containment Lower Compartment 
    temperature will not change the operation of any equipment which is 
    important to safety. All components and instruments will continue to 
    perform as designed in the higher temperature environment for the 
    period that the revised Technical Specification allows. This 
    temperature increase will not impact the ability of any component or 
    instrument to perform its function in the event of an accident. 
    Therefore, the probability of an accident is not impacted. The 
    increased temperature will cause a decrease in the air mass in lower 
    containment. This change has been evaluated for impact on 
    containment temperature and pressure in accident conditions. The air 
    mass change is conservative for peak containment pressure since the 
    air mass is decreased. Maximum containment temperatures during a 
    postulated accident are slightly increased as a result of higher 
    initial Containment Lower Compartment temperature. The increase in 
    peak temperature remains within the allowable values and thus does 
    not increase the probability or consequence of an accident. The 
    minimum containment pressure as a result of steam condensation in 
    containment is lowered as a result of the decreased air mass in 
    containment. Due to the conservative assumptions made in modeling 
    containment for minimum pressure response, this change has no impact 
    on the accident analysis.
        Based on the analysis of the bounding accidents that may be 
    impacted by increased Containment Lower Compartment temperature and 
    the review of the effect of the increased temperature on components 
    in lower containment, it is determined that the probability and 
    consequence of any analyzed accident is unchanged as a result of 
    this change.
        2. Does the proposed amendment create the possibility of a new 
    or different kind of accident not previously evaluated?
        The revised maximum Containment Lower Compartment temperature 
    will not change any systems or operations procedures except to 
    procedurally respond should Containment Lower Compartment 
    temperature remain elevated for a period near the revised limiting 
    period. The response of the systems and components are unaffected by 
    this change. All instruments are qualified for the revised service 
    conditions and will perform in the same manner as before. Normal 
    operation and transient response will remain unchanged. Review of 
    previously analyzed accidents show that no new transients are 
    created as a result of this change. Based on this review there are 
    no new or different accidents made possible by this change.
        3. Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        The amendment could potentially affect the containment system. 
    The operation and analysis of the reactor coolant system and fuel 
    are unaffected by this change. The maximum containment temperature 
    is slightly increased while the maximum containment pressure is 
    decreased. The minimum containment pressure could be slightly 
    decreased and minimum containment temperature is unaffected. All 
    these parameters have been reviewed and determined to be within 
    assumptions made in these analyses. The accident transient analyses 
    are unaffected beyond these small changes and remains acceptable in 
    all cases. Therefore, the margin of safety is unaffected by this 
    amendment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, North Carolina 28223-0001
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: January 6, 1997
        Description of amendment request: The proposed amendments would 
    allow a one-time revision to Technical Specifications 3.6.1.1, 3.6.1.2, 
    3.6.1.8, and 3.6.1.9 to allow operation of the Containment Purge 
    Ventilation System (VP) during Modes 3 and 4 following the steam 
    generator (SG) replacement outage. This one-time revision would be 
    necessary due to respiratory hazardous gases released during heatup 
    after the replacement of the SGs. The VP system would be used to remove 
    the hazardous gases.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. The activity does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The VP [Containment Purge Ventilation] System has no interfaces 
    with any primary system, secondary system, or power transmission 
    system. It has no interfaces with any reservoir of radioactive gases 
    or liquids. None of the systems listed above are modified by the 
    activity. In summary, no ``accident initiator'' is affected with the 
    proposed operation of the VP System in Modes 3 and 4. For this 
    reason, the activity does not involve an increase in the probability 
    of an accident previously evaluated.
        Analyses have been performed to determine upper bounds to the 
    source term, the offsite doses, and the Control Room dose. The 
    results of that analyses are reported above. Both the source term 
    and the doses were found to be significantly lower than the results 
    of the corresponding design basis analyses. In addition, it has been 
    determined that with no credit taken for any heat transfer from the 
    fuel and cladding to the moderator channels, that sufficient time 
    would exist for the operators to initiate recovery of flow from the 
    ECCS [Emergency Core Cooling System] to the reactor core. The flow 
    required from the ECCS to maintain the core in a coolable geometry 
    was found to be well within the capacity of any one ECCS pump. 
    Furthermore, it was determined that convective heat transfer to 
    steam would be sufficient to prevent release of significant source 
    term or a significant degree of fuel damage.
        For the above reasons, it is determined that operation of the VP 
    System in Mode 3 or 4 immediately following the steam generator 
    replacement outage does not involve a significant increase in either 
    the probability or the consequences of an accident previously 
    evaluated.
        2. The activity does not create the possibility of a new or 
    different type of
    
    [[Page 6575]]
    
    accident from any accident previously evaluated.
        As discussed above, no ``accident initiators'' are affected by 
    the proposed activity. Operation of the VP System proposed for Modes 
    3 and 4 will be the same as that routinely carried in other modes of 
    operation. For these reasons, the activity will not create the 
    possibility of a new or different type of accident from any 
    previously evaluated.
        3. The activity does not involve a significant reduction in the 
    margin of safety.
        Margin of safety is associated with confidence in the ability of 
    the fission product barriers (the fuel and fuel cladding, the 
    Reactor Coolant System pressure boundary, and the containment) to 
    limit the level of radiation doses to the public. The proposed 
    operation of the VP System will occur at the end of an extended 
    outage. The level of decay heat and activity in the reactor is very 
    low compared to the level of decay heat and activity associated with 
    full power operations. For this reason, the likelihood of damage to 
    the fuel following a DBLOCA [design basis loss-of-coolant accident] 
    occurring during the proposed purging is reduced, as determined 
    above. Both offsite doses and doses to the Control Room were found 
    to be small compared to the limits of 10 CFR [Part] 100 and GDC 
    [General Design Criterion] 19. For these reasons, the activity does 
    not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, North Carolina 28223-0001
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: January 13, 1997
        Description of amendment request: The proposed amendments would 
    implement the performance-based containment leak rate testing 
    requirements of 10 CFR Part 50, Appendix J, Option B, for Type A 
    testing.
        Compliance with 10 CFR Part 50, Appendix J, provides assurance that 
    the primary containment, including those systems and components that 
    penetrate the primary containment, do not exceed the allowable leakage 
    rate values specified in the Technical Specifications and Bases. The 
    allowable leakage rate is determined so that the leakage assumed in the 
    safety analyses is not exceeded.
        On February 4, 1992, the NRC published a notice in the Federal 
    Register (57 FR 4166) discussing a planned initiative to begin 
    eliminating requirements marginal to safety that impose a significant 
    regulatory burden. Appendix J to 10 CFR Part 50, ``Primary Containment 
    Leakage Testing for Water-Cooled Power Reactors,'' was considered for 
    this initiative and the staff undertook a study of possible changes to 
    this regulation. The study examined the previous performance history of 
    domestic containments and examined the effect on risk of a revision to 
    the requirements of Appendix J. The results of this study are reported 
    in NUREG-1493, ``Performance-Based Leak-Test Program.''
        Based on the results of this study, the staff developed a 
    performance based approach to containment leakage rate testing. On 
    September 12, 1995, the NRC approved issuance of this revision to 10 
    CFR Part 50, Appendix J, which was subsequently published in the 
    Federal Register on September 26, 1995, and became effective on October 
    26, 1995. The revision added Option B ``Performance-Based 
    Requirements'' to Appendix J to allow licensees to voluntarily replace 
    the prescriptive testing requirements of Appendix J with testing 
    requirements based on both overall and individual component leakage 
    rate performance.
        Regulatory Guide 1.163, ``Performance-Based Containment Leak Test 
    Program,'' was developed as a method acceptable to the staff for 
    implementing Option B. Accordingly, the licensee has submitted, in its 
    application dated January 13, 1997, proposed changes to the TS to 
    implement 10 CFR Part 50, Appendix J, Option B, by referring to 
    Regulatory Guide 1.163, ``Performance-Based Containment Leakage-Test 
    Program.''
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. The proposed change will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Containment leak rate testing is not an initiator of any 
    accident; the proposed change does not affect reactor operations or 
    accident analysis, and has no significant radiological consequences. 
    ... Therefore, this proposed change will not involve an increase in 
    the probability or consequences of any previously-evaluated 
    accident.
        2. The proposed change will not create the possibility of any 
    new accident not previously evaluated.
        The proposed change does not affect normal plant operations or 
    configuration, nor does it affect leak rate test methods. The test 
    history at McGuire (two consecutive successful tests) provides 
    continued assurance of the leak tightness of the containment 
    structure.
        3. There is no significant reduction in a margin of safety.
        The proposed changes are based on NRC-accepted provisions, and 
    maintain necessary levels of reliability of containment integrity. 
    The performance-based approach to leakage rate testing recognizes 
    that historically good results of containment testing provide 
    appropriate assurance of future containment integrity; this supports 
    the conclusion that the impact on the health and safety of the 
    public as a result of extended test intervals is negligible. In 
    addition, local leak[]rate testing will continue to provide 
    assurances of overall containment integrity.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, North Carolina 28223-0001
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: October 16, 1996
        Description of amendment request: The amendment requests to change 
    the Waterford 3 Technical Specifications Table 4.3-1 to expand the 
    applicability for Core Protection Calculator operability and to allow 
    for the application of a Cycle Independent Shape Annealing Matrix.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        The proposed change will reduce the amount of non-conservatism 
    presently allowed for linear power level, the CPC delta T power, and 
    CPC nuclear power signals.
    
    [[Page 6576]]
    
    Changing the tolerance range from plus or minus 2% to between -0.5% 
    and 10% between 15% and 80% RATED THERMAL POWER, except during 
    physics testing, will allow more conservative settings than 
    currently allowed. The consequences of an accident will be reduced 
    due to the proposed change because it is less likely to be non-
    conservative in power.
        This proposed change will allow use of Cycle Independent Shape 
    Annealing Matrix (CISAM) elements. These elements will be validated, 
    during startup testing, by monitoring the same parameters used for 
    cycle specific shape annealing matrix (SAM) elements. If the CISAM 
    is determined to be no longer valid, a cycle specific SAM will be 
    calculated and used in the CPC's. In addition, use of CISAM gives 
    better agreement throughout the cycle.
        Therefore, the proposed changes will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        The proposed change to TS power calibration tolerance limits is 
    conservative relative to the current TS requirement. CPC's cannot 
    cause an accident and this change will not create the possibility of 
    a new or different type accident. The changes ensures that the 
    reactor will trip prior to the current condition due to higher CPC 
    power.
        As stated previously, CISAM modeling removes some of the 
    uncertainty associated with axial shape and provides increased 
    assurance that the CPC is appropriately modeling the core.
        Therefore, the proposed changes will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        The proposed change to the TS reduces the amount of non-
    conservatism in safety system power indications and maintains the 
    margin of safety for design basis events which take credit for the 
    linear power level, the CPC delta T power, and CPC nuclear power 
    signals.
        CISAM will be validated each cycle during startup testing and 
    must meet the same parameters as cycle specific SAM elements. Since 
    CISAM has a better accuracy than the cycle dependent SAM, the margin 
    of safety is improved.
        Therefore, the proposed changes will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: November 27, 1996
        Description of amendment request: The proposed change request would 
    change the acceptance criteria for the individual cell voltage from 
    2.0v to 2.09v, change the surveillance frequency for battery specific 
    gravities to implement the recommendations of IEEE 450-1995, delete 
    surveillance requirement 4.7.B.4.d, add a clarifying phrase ``while on 
    a float charge....'' where appropriate, and update the Basis to reflect 
    these changes.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        This request has been determined to involve No Significant 
    Hazards in that it does not:
        1. Involve a significant increase in the probability or 
    consequences
        of an accident previous[ly] evaluated; (or)
        The proposed change in ICVs [individual cell voltages] does not 
    increase the probability of an accident previously evaluated, as it 
    increases the required voltage for each ICV.
        The proposed change in frequency does not increase the 
    probability or consequences of an accident previously evaluated, as 
    the change in the frequency of specific gravity testing is the 
    result of industry experience gained over the years. The weekly 
    reading of pilot cell specific gravity and cell voltage, along with 
    the quarterly reading of all ICVs and a 10% sample of specific 
    gravities from designated cells provides an acceptable means of 
    determining cell operability as specified in IEEE 450-1995.
        The proposed deletion of Technical Specification Surveillance 
    Requirement 4.7.B.4.d only removes an unnecessary Technical 
    Specification surveillance and is consistent with NUREG-1433, 
    Standard Technical Specifications General Electric Plants, BWR/4, 
    Revision 1, April 1995. No change to plant systems, components or 
    operating conditions are associated with this change. Existing 
    Technical Specification station and diesel generator battery 
    inspection and testing requirements adequately verify battery 
    operability and condition.
        2. Create the possibility of a new or different kind of accident 
    from any accident previous[ly] evaluated; (or)
        The proposed change does not create the possibility of a new or 
    different kind of accident than previously evaluated, as the change 
    only involves raising a required voltage, performing an existing 
    surveillance on a different frequency, and removing an unnecessary 
    annunciator surveillance requirement. The station battery and diesel 
    generator battery low voltage annunciator setpoints do not meet any 
    of the criteria codified in 10 CFR 50.36 for determining content of 
    Technical Specifications and removal of surveillance requirement is 
    consistent with NUREG-1433, Standard Technical Specifications 
    General Electric Plants, BWR/4, Revision 1, April 1995. There is no 
    change to hardware or operating conditions.
        3. Involve a significant decrease in the margin of safety.
        The proposed change to the ICV does not decrease the margin of 
    safety, as increasing the required voltage actually increases the 
    margin of safety. The proposed change to the frequency does not 
    decrease the margin of safety as it continues to require testing and 
    evaluation of the requisite surveillance points and implements 
    requirements which have been determined to provide an adequate level 
    of safety by the IEEE. The removal of Technical Specification 
    surveillance requirements for the battery low voltage annunciator 
    setpoints does not affect any plant systems, components or operating 
    conditions.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Patrick D. Milano, Acting
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: January 23, 1997, as revised by letter 
    dated January 28, 1997.
        Description of amendment request: The proposed amendment would make 
    changes to Section 3.5/4.5.C of the technical specification (TS) bases 
    to clarify the minimum residual heat removal (RHR) and residual heat 
    removal service water (RHRSW) pump requirements for post-accident 
    containment heat removal. In conjunction with the proposed amendment, 
    the licensee requested NRC staff review and approval of an update to 
    the design basis accident containment temperature and pressure response 
    for the limiting single failure (loss of diesel generator) which 
    results in minimum RHR and RHRSW pump availability.
        Basis for proposed no significant hazards determination: As 
    required by
    
    [[Page 6577]]
    
    10 CFR 50.91(a), the licensee has provided its analysis of the issue of 
    no significant hazards consideration. The NRC staff has reviewed the 
    licensee's analysis against the standards of 10 CFR 50.92(c). The NRC 
    staff's review is presented below.
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed amendment will change TS bases to clarify the 
    minimum RHR and RHRSW pump requirements for post-accident 
    containment heat removal. The proposed amendment will also correct 
    an error in a previous analysis on containment temperature and 
    pressure response following a design basis accident (DBA) that was 
    submitted for the NRC staff review on May 1, 1986. The proposed 
    amendment does not affect the physical configuration of the plant or 
    how it is operated. The licensee's analysis, using a new decay heat 
    model, determined that the calculated maximum suppression pool 
    temperature will be 2 degrees Fahrenheit greater (184 degrees 
    Fahrenheit vs. 182 degrees Fahrenheit) than that predicted in its 
    previous analysis, based on an earlier decay heat model, that was 
    submitted for the NRC staff review on May 1, 1986. The licensee 
    evaluated the effects of this increase on emergency core cooling 
    system (ECCS) pump net positive suction head, wetwell attached 
    piping, and environmental conditions in the ECCS pump rooms, and 
    concluded that the change is acceptable. The consequences or 
    probability of a previously evaluated accident will, therefore, not 
    be significantly increased.
        (2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment does not create the possibility of a new or 
    different kind of accident from any previously evaluated since the 
    proposed amendment does not affect the physical configuration of the 
    plant or how it is operated. The proposed amendment revises the TS 
    bases to clarify the minimum RHR and RHRSW pump requirements for post-
    accident containment heat removal.
        (3) The proposed changes do not result in a significant 
    reduction inthe margin of safety.
        The proposed amendment will change TS bases to clarify the 
    minimum RHR and RHRSW pump requirements for post-accident 
    containment heat removal. The proposed amendment will also correct 
    an error in a previous analysis on containment temperature and 
    pressure response following a design basis accident (DBA) that was 
    submitted for the NRC staff review on May 1, 1986. The proposed 
    amendment does not affect the physical configuration of the plant or 
    how it is operated. The licensee's analysis, using a new decay heat 
    model, determined that the calculated maximum suppression pool 
    temperature will be 2 degrees Fahrenheit greater (184 degrees 
    Fahrenheit vs. 182 degrees Fahrenheit) than that predicted in its 
    previous analysis, based on an ealier decay heat model, that was 
    submitted for the NRC staff review on May 1, 1986. The licensee 
    evaluated the effects of this increase on emergency core cooling 
    system (ECCS) pump net positive suction head, wetwell attached 
    piping, and environmental conditions in the ECCS pump rooms, and 
    concluded that the change is acceptable. Therefore, the proposed 
    amendment does not involve a significant reduction in a margin of 
    safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW. Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: December 9, 1996
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant (DCPP) Unit Nos. 1 and 2 to revise the surveillance 
    frequencies from at least once every 18 months to at least once per 
    refueling interval (nominally 24 months) for the reactor trip system 
    (RTS) and engineering safety features actuation systems (ESFAS) 
    instrumentation channels, and make certain changes in trip setpoints 
    and allowance values due to a setpoint methodology change in support of 
    the calibration extensions. Channel operational tests (COTs) and trip 
    actuating device operational tests (TADOTs) associated with these 
    channels are also being extended. Revisions to the appropriate TS Bases 
    are being revised to support the TS revisions.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed TS channel calibration, COT, and TADOT interval 
    increases from 18 to 24 months, the setpoint change, and the 
    allowable value changes do not alter the intent or method by which 
    the channel calibrations are conducted, do not alter the way any 
    structure, system, or component functions, and do not change the 
    manner in which the plant is operated. The calibration and 
    maintenance histories indicate that the equipment will continue to 
    perform satisfactorily with longer surveillance intervals. With the 
    exception of the pressurizer water level - high instrument, no 
    recurring surveillance or maintenance problems were identified for 
    the RTS or ESFAS instrumentation channels.
        The pressurizer water level instruments do not have a safety 
    limit and are not credited in the DCPP safety analysis. The 
    recurring surveillance problems were mainly due to calibration zero 
    shift which is reflected in the statistically determined drift and 
    in the proposed pressurizer water level high setpoint. The zero 
    shift problem of these transmitters was a recurring problem with the 
    calibration procedure. The procedures for calibrating these 
    instruments have been revised to improve the repeatability of the 
    surveillance activity.
        The trip setpoint and allowable value changes for pressurizer 
    water level - high are each in the more restrictive direction. The 
    revised setpoint would tend to trip the reactor sooner than the 
    present settings. These changes ensure that sufficient margin is 
    maintained for the pressurizer water level to accommodate the 
    channel statistical uncertainty resulting from a 30-month operating 
    cycle.
        A statistical analysis of channel uncertainty for a bounding 30-
    month operating cycle has been performed. There is sufficient margin 
    between the existing TS limits and the licensing basis safety 
    analysis limits to accommodate the channel statistical uncertainty 
    resulting from a 30-month operating cycle. The existing margin 
    between the TS limits and the safety analysis limits provides 
    assurance that plant protective actions will occur as required. 
    However, a change to the safety analysis limit is proposed in order 
    to provide additional margin for the RCS loss of [f]low-low 
    setpoint.
        Westinghouse has evaluated the safety analysis limit for the RCS 
    loss of flow-low setpoint and has determined that the limit can be 
    changed from 87 percent of MMF to 85 percent of MMF with no impact 
    on the probability and insignificant impact on the consequences of 
    accidents already analyzed. The existing conclusions of the DCPP 
    FSAR Update remain valid with the safety analysis limit change. 
    Using the new safety analysis limit, sufficient margin exists 
    between the TS limit and the safety analysis limit to accommodate 
    the channel statistical uncertainty resulting from a 30-month 
    operating cycle.
        The proposed changes to the allowable values ensure that drift 
    assumptions regarding the protection racks and direct input 
    functions are met.
        There are no known mechanisms that would significantly degrade 
    the performance of the evaluated instrument channels during normal 
    plant operation. All potential time-
    
    [[Page 6578]]
    
     related degradation mechanisms have insignificant effects in the 
    time frame of interest (maximum of 30 months). PG&E will continue to 
    perform the maintenance required to maintain the qualification of 
    this safety related equipment.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed pressurizer water level trip setpoint, RCS flow 
    safety analysis limit, and various allowable value changes provide 
    adequate margin to accommodate instrument channel uncertainty over a 
    30-month operating cycle. Plant equipment, which will be set at, or 
    more conservative than, the trip setpoints, will provide protective 
    functions to assure that the safety analysis limits are not 
    exceeded. The change to the RCS loss of flow safety analysis limit 
    does not create the possibility of a new or different kind of 
    accident since the setpoint will remain as currently specified and 
    only results in an insignificant delay in the plant response to the 
    accident.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        For almost all the existing DCPP RTS/ESFAS setpoints, the 
    existing difference between the safety analysis limit and the 
    setpoints was sufficient to accommodate any changes in instrument 
    uncertainty.
        The change in the pressurizer water level - high setpoint does 
    not affect a safety analysis limit and, therefore, has no effect on 
    a margin to safety. Since the normal pressurizer level is maintained 
    at 60 percent span and the no-load Tavg control level is 22 
    percent span, a change in the setpoint from less than or equal to 92 
    percent span to less than or equal to 90 percent span is not 
    significant to either DCPP plant operation or safety.
        The change in the RCS loss of flow-low safety analysis limit 
    from 87 percent MMF to 85 percent MMF does not affect the existing 
    plant setpoint and was evaluated to have a negligible effect on the 
    limiting conditions of a partial loss of flow accident, a single RCP 
    locked rotor, or RCP shaft break accident. This safety limit change 
    was also found to have no effect on the DCPP minimum DNBR since the 
    minimum DNBR is associated with the complete loss of flow accident. 
    The complete loss of flow accident was evaluated to the Condition II 
    fault criteria applicable to the partial loss of flow accident 
    evaluation and was acceptable.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: December 23, 1996
        Description of amendment request: The proposed amendment would 
    allow the use of Vantage Plus fuel.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed?
        The probability of occurrence or the consequences of an accident 
    previously evaluated is not significantly increased. The VANTAGE + 
    fuel assemblies containing ZIRLOTM clad fuel rods, thimble and 
    instrument tubes, IFMs, [intermediate fuel mixing assemblies] and 
    LPD [low-pressure-drop] mid-grids meet the same fuel assembly and 
    fuel rod design bases as VANTAGE 5 (without IFMs) fuel assemblies in 
    the other fuel regions. In addition, the 10 CFR 50.46 criteria will 
    be applied to the ZIRLOTM clad fuel rods, thimble and 
    instrument tubes, IFM grids, and LPD mid-grids. The use of these 
    fuel assemblies will not result in a change to the proposed Indian 
    Point Unit 3 VANTAGE 5 (without IFMs) transition core design and 
    safety analysis limits. The ZIRLOTM clad material is similar in 
    chemical composition and has similar physical and mechanical 
    properties as that of Zircaloy-4. Thus the cladding integrity is 
    maintained and the structural integrity of the fuel assembly is not 
    affected. The ZIRLOTM clad fuel rod improves corrosion 
    resistance and dimensional stability. In addition, the incorporation 
    of LPD mid-grids and IFMs improves dimensional stability. Since the 
    dose predictions in the safety analyses are not sensitive to the 
    fuel assemblies material changes as specified in this report, the 
    radiological consequences of accidents previously evaluated in the 
    safety analyses remain valid. Therefore, the probability or 
    consequences of an accident previously evaluated is not 
    significantly increased.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        The possibility for a new or different type of accident from any 
    accident previously evaluated is not created, since the VANTAGE + 
    fuel assemblies containing ZIRLOTM clad fuel rods, thimble, and 
    instrument tubes, IFMs, and LPD mid-grids will satisfy the same 
    design bases as that used for VANTAGE 5 (w/o IFMs) fuel assemblies 
    in the other fuel regions. Since the original design criteria is 
    being met, the ZIRLOTM clad fuel rods, thimble and instrument 
    tubes, IFMs, and LPD mid-grids will not be an initiator for any new 
    accident. All design and performance criteria will continue to be 
    met and no new single failure mechanisms have been created. In 
    addition, the use of these fuel assemblies does not involve any 
    alterations to plant equipment or procedures which would introduce 
    any new or unique operational modes or accident precursors. 
    Therefore, the possibility for a new or different kind of accident 
    from any accident previously evaluated is not created.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        The margin of safety is not significantly reduced, since the 
    VANTAGE + fuel assemblies containing ZIRLOTM clad fuel rods, 
    thimble and instrument tubes; IFMs, and LPD mid-grids do not change 
    the proposed Indian Point 3 VANTAGE 5 (w/o IFMs) transition core 
    design and safety analysis limits. The use of these fuel assemblies 
    containing fuel rods, thimble and instrument tubes with ZIRLOTM 
    cladding alloy; IFMs and LPD mid-grids will take into consideration 
    the normal core operating conditions allowed in the Technical 
    Specifications. For the transition core and each future cycle reload 
    core, these fuel assemblies will be specifically evaluated using 
    standard reload design methods and approved fuel rod design models 
    and methods. This will include consideration of the core physics 
    analysis, peaking factors and core average linear heat rate effects. 
    In addition, the 10 CFR 50.46 criteria will be applied each cycle to 
    the ZIRLOTM clad fuel rods, thimble and instrument tubes, IFMs, 
    and LPD mid-grids. Analyses or evaluations will be performed each 
    cycle to confirm the 10 CFR 50.46 will be met. Therefore, the margin 
    of safety as defined in the Bases to the Indian Point Unit 3 
    Technical Specifications and VANTAGE 5 (w/o IFMs) ZIRLOTM 
    licensing amendment approval is not significantly reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: S. Singh Bajwa, Acting
    
    [[Page 6579]]
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: July 9, 1996 (TXX-96393)
        Brief description of amendments: The proposed changes would 
    increase the minimum allowable value of the Unit 1 Steam Line Pressure-
    -Low Safety Injection and Steam Line Isolation functions. These changes 
    are needed to ensure that the instrumentation error is properly 
    accounted for in the Technical Specifications.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The changes in the License Amendment Request proposes more 
    restrictive setpoint Allowable Values for the Steam Line pressure--
    Low channels of the Engineered Safety Features Actuation System 
    (ESFAS). These more restrictive values assure that all applicable 
    safety analysis limits are being met. Changing an Allowable Value in 
    the Technical Specifications has no impact on the probability of 
    occurrence of any accident previously evaluated. None of the 
    accident analyses were affected, therefore, the consequences of all 
    previously evaluated accidents remain unchanged.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed changes involve the use of a more conservative 
    value for the Allowable Value for the Steam Line Pressure--Low 
    Safety Injection and Steam Line Isolation functions. As such, none 
    of the changes effect plant hardware or the operation of plant 
    systems in a way that could initiate an accident. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        There were no changes made to any of the accident analyses or 
    safety analysis limits as a result of this proposed change. Further, 
    the proposed change does not affect the acceptance criteria for any 
    analyzed event. ESFAS will remain capable of performing its safety 
    function, and the new requirement will continue to provide adequate 
    assurance of that capability. Making the Allowable Value more 
    restrictive provides increased assurance that the channels will 
    function within the safety analysis limits assumed in the safety 
    analyses. The margin of safety established by the Limiting 
    Conditions for Operation also remains unchanged. Thus there is no 
    effect on the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: July 10, 1996 (TXX-96405), as 
    supplemented by letter dated October 1, 1996 (TXX-96475)
        Brief description of amendments: The proposed change would take 
    credit for the addition of train oriented Fan Coil Units for each UPS & 
    Distribution Room and would provide redundancy to the existing Air 
    Conditioning Units.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The UPS HVAC System is a support system for other safety related 
    equipment, primarily the Uninterruptible Power Supplies and some of 
    their distribution equipment. The only impact that this system can 
    have on the probability or consequences of an accident must result 
    from the failure of the system to provide adequate support to the 
    supported safety related equipment when that supported safety 
    related equipment is required to operate.
        Allowing same train cooling to satisfy the LCO is considered 
    equivalent to the existing Technical Specification. The proposed 
    changes allow the use of the same train UPS Room Fan Coil Units or 
    the same train UPS A/C Train to support a UPS & Distribution Room.
        Surveillance requirements are added or modified to ensure that 
    the credited support equipment will be available when needed. 
    Unnecessary starts of the UPS A/C Trains have been eliminated from 
    the specifications. Overall, this is considered an enhancement that 
    will increase the reliability of the UPS HVAC Systems. Because both 
    the existing specification and the proposed revision to the 
    specification continue to ensure normal support and the availability 
    of at least one train of equipment in the event of a design basis 
    accident, with the same or increased reliability, the consequences 
    of an accident previously evaluated is not affected.
        Changing the specification from a ``common'' specification which 
    impacts both units simultaneously to a specification which applies 
    to both units separately is basically just an administrative change. 
    Having ``common'' specifications is an aid to the operator to 
    provide an alert that both units are affected. With the new LCO, 
    both units may not be affected because rooms may now be cooled 
    separately. Because both CPSES Units remain properly covered, 
    however, this change will not significantly increase the probability 
    of consequences of an accident.
        The revision to the existing ACTION is considered equivalent 
    except for the change of the Allowed Outage Time (AOT) from seven 
    days to 30 days. This change is based on the significance of the 
    heating and cooling function but does represent an increase in AOT 
    and thus an increase in the probability that the supported functions 
    could be unavailable. This increase is not considered significant 
    based on the following several factors:
        a)the systems design is based on a conservative assessment of 
    the worst postulated conditions in the rooms;
        b) generally, less than design cooling is required and a short 
    duration or partial failure may have little or no impact on the 
    systems ability to perform its function;
        c) the multiple backups available (two UPS A/C Trains and only 
    one UPS Room Fan Coil Unit per each room) increase the potential of 
    restoring additional cooling if needed;
        d) the ability to perform alternate actions if normal cooling is 
    lost such as circulating air via existing fans or portable fans 
    thereby extending the time before cooling must be restored; and
        e) the extended AOT would allow more time and opportunity to 
    perform corrective maintenance to ensure high equipment reliability.
        The new ACTION for loss of cooling reflects requirements that 
    already exist in the Technical Specifications. The AOT for this 
    ACTION statement is 72 hours which is based on the risk from an
        event occurring requiring the inoperable UPS A/C Train, and the 
    remaining UPS Room Fan Coil Units and A/C Train fans providing the 
    required protection.
        The new ACTION for loss of cooling and ventilation reflects a 
    conservative response to the potential impact of such a condition. 
    The proposed AOT is one hour. One hour is based on the time lag 
    available from the operating temperature to the maximum Technical 
    Specification limit of the UPS & Distribution Rooms. The addition of 
    a specific ACTION in lieu of relying on Specification 3.0.3, 
    although essentially equivalent, is consistent with the methodology 
    of the improved Standard Technical Specifications and alerts the 
    operator to the significance of the situation.
        The changes made to the surveillance ensure that the UPS Room 
    Fan Coil Units will operate. The UPS Room Fan Coil Units are 
    connected to the emergency busses and TS 4.8.1.1.2f. demonstrates 
    the energization of emergency busses with permanently connected 
    loads. The changes made to the 18
    
    [[Page 6580]]
    
    month surveillances on the UPS A/C trains were changed from the 
    Safety Injection signal with the Blackout Test signal to ``... 
    actual or simulated actuation signal''. This is consistent with 
    NUREG-1431, ``Standard Technical Specifications Westinghouse 
    Plants''.
        The changes to the BASES are descriptive in nature to reflect 
    the other changes and by themselves have no impact on the 
    probability or consequences of an accident.
        The ability to cope with station blackout and design basis fires 
    is maintained or enhanced. For station blackout coping, the UPS A/C 
    fans are considered to remain available while additional cooling is 
    provided by a single available Fan Coil Unit.
        In summary, the proposed changes take advantage of the increased 
    reliability offered by the revised system design. It also maintains 
    the level of support provided by the system while at worst, allowing 
    a slight decrease in availability (in certain situations) which is 
    not considered significant. As a result, it is concluded that none 
    of the changes made to the existing Technical Specification involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any previously evaluated?
        Revising this specification to take credit for the new UPS Room 
    Fan Coil Units, to take credit for same train UPS A/C Train support 
    for a UPS and Distribution Room, to make the specification unit 
    specific instead of common, to make the surveillances appropriate 
    for the credited equipment, and to make the action statements 
    appropriate for the credited equipment and their significance, does 
    not by itself alter plant hardware. Plant procedures are only 
    altered to the extent that the revised specification will allow 
    different configurations of equipment in the UPS HVAC System to be 
    operated at different times. These changes ensure continued support 
    of the safety related equipment in the affected areas and do not 
    affect the equipments failure or failure modes. As a result, these 
    changes to the Technical Specification do not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        None of the changes being proposed alter the environmental 
    conditions which are to be maintained in the areas supported by an 
    OPERABLE UPS HVAC System during normal operations and following an 
    accident. As a result, the margin of safety for these functions 
    remains the same. The only potential adverse impact is the system's 
    postulated availability, as discussed in the response to question 1 
    above. This reduction in availability is to a great extent mitigated 
    by the projected increase in system reliability. As noted in the 
    response to question 1, there is no significant impact on the 
    accident analyses. Thus, even if system availability issues were 
    considered an aspect of margin of safety, the proposed changes do 
    not involve a significant reduction in margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: December 17, 1996
        Description of amendment request: The proposed changes will allow 
    one of the two service water loops to be isolated from the component 
    cooling water heat exchangers (CCHXs) during power operation in order 
    to refurbish sections of the isolated service water headers. The 
    proposed temporary changes will be valid for two periods of up to 35 
    days each for implementation of the service water upgrades associated 
    with the repair of the sections of the 24-inch service water supply and 
    return piping to/from the CCHXs.
        Basis for proposed no significant hazards determination: As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
        Specifically, operation of North Anna Power Station in 
    accordance with the proposed Technical Specifications changes will 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The piping refurbishment project and the proposed temporary 
    changes to the SW [service water] and CC [component cooling] 
    Technical Specifications have been evaluated to assess their impact 
    on the normal operation of the SW and CC systems and to ensure that 
    the design basis safety functions of each system are preserved. The 
    SW system is required to function during all normal and emergency 
    operating conditions. During normal plant operation, the SW system 
    provides cooling water to the CCHXs, charging pump coolers, 
    instrument air compressor coolers, and control room chiller 
    condensers of both units. Within the first 168 hour Section 3/
    4.7.4.1.d TS AS [Action Statement] of isolation of the header which 
    is to be repaired, temporary 10'' diameter SW lines (one supply and 
    one return) will be installed to supply the SW to the charging pumps 
    coolers, instrument air compressors coolers, Unit 2 CR chillers and 
    spent fuel pool (SFP) coolers to satisfy design basis conditions. 
    These temporary lines will be routed from the operating part of the 
    36'' SW headers while the 24'' headers to CCHXs are being repaired. 
    The temporary lines will be dismantled when the repaired header is 
    returned to operation (second 168 hour AS). During the two 35-day 
    periods, one header will operate with its 24-inch piping to/from the 
    CCHXs temporarily blanked. To avoid operation of the SW pump at 
    abnormal conditions (low flow) on this ``partially deadlocked'' 
    header, a temporary cross-connect will be installed to by-pass the 
    CCHXs.
        SW system operation with the cross-connect installed was 
    evaluated for design basis accident (DBA) conditions. The DBA 
    condition for the SW system is a loss-of-coolant accident on one 
    unit with simultaneous loss-of-offsite-power to both units. [An] SW 
    system hydraulic analysis has been performed to verify that adequate 
    flow is provided to the containment recirculation spray heat 
    exchangers (RSHXs) with the temporary cross-connect installed and 
    throttled open, assuming the occurrence of the most limiting single 
    failure. Therefore, there is no increase in probability or 
    consequences of the DBA condition.
        Utilizing only one SW header to supply flow to the CCHXs has the 
    potential to affect the reliability of the CC system and all of the 
    equipment cooled by CC. A review of the equipment affected by this 
    phase of the SW restoration project was performed to evaluate the 
    impact on initiating event frequency. Since the SW system and CC 
    system are support systems used to remove heat, a failure in either 
    of these systems does not affect the initiating event frequency of 
    any design basis event. Additionally, an estimate of the impact on 
    core damage frequency is provided below. The impact on the North 
    Anna Probabilistic Safety Assessment (PSA) during implementation of 
    this DCP [design change package] is similar to impact of work 
    performed under DCP-94-010 since the scope of work of both DCPs is 
    repair/replacement of different portions of the same 24'' SW headers 
    to CCHXs. The only difference from a PSA standpoint is that CDF 
    [core damage frequency] for DCP-94-010 was calculated based on 140 
    days supply of CCHXs from one SW header while per this DCP it is 
    only 70 days. Therefore, results of PSA evaluation for DCP-94-010 
    are conservatively applied to this DCP. The activities to be 
    performed during the refurbishment project and the various system 
    alignments required have been evaluated using the Individual Plant 
    Examination (IPE) Probabilistic Safety Assessment (PSA) model for 
    North Anna Power Station. This model is used in a manner that is 
    generally consistent with the Electric Power Research Institute 
    (EPRI) PSA Applications Guide TR-105396. The effect on the PSA model 
    is a slight increase in the frequency of reactor trips and an 
    increase in the probability of RHR [residual heat removal] failure.
        The increased frequency of reactor trips is due to the decreased 
    reliability of the CC system to supply cooling to the RCP [reactor 
    coolant pump] motor. When only one SW header is available to the CC 
    heat exchangers
    
    [[Page 6581]]
    
    the frequency of losing this single header is dominated by the 
    probability of both SW pumps failing. Also considered was the 
    frequency of pipe rupture anywhere in the single available header. 
    When the single SW header fails to supply cooling to the CC heat 
    exchangers, the CC system will heatup causing inadequate cooling for 
    sustained operation of the RCPs. Tripping these pumps results in a 
    reactor trip. The second SW header can be expected to supply other 
    equipment with cooling. This scenario is appropriately modeled as a 
    reactor trip with main feedwater available initiating event. A 
    sensitivity analysis shows the increase in CDF to be about 1E-8/
    year. The total effect of this DCP includes a failure analysis of 
    the reactor coolant pump and motor in case of loss of CCW.
        The CC system is also included in the PSA model as a support 
    system for RHR cooling. The RHR system is used to reduce reactor 
    coolant system temperatures from 350 deg.F (hot shutdown) to 
    140 deg.F (cold shutdown). The only accident initiator that requires 
    the unit to be cooled down and placed on RHR cooling are sequences 
    which are initiated with a steam generator tube rupture. (Note that, 
    for the North Anna plant design, RHR is separate from the safety 
    injection system and the low head safety injection pumps.) The 
    increased probability for the loss of RHR when only one SW header is 
    available to the CCHXs is estimated using fault tree analysis and is 
    dominated by the failure of both SW pumps. The probability for the 
    loss of both SW pumps aligned to the CCHXs is estimated to be 1.5E-
    4. The effect of this increase in RHR failure probability was 
    determined by adding this probability to the top single event in the 
    RHR function and recalculating the new CDF. The resulting increase 
    in CDF as a result of RHR system failure following a steam generator 
    tube rupture is less than 1E-8 per year.
        The CC system is further included in the PSA model as part of 
    the loss of RCP seal cooling as an initiating event and as a loss of 
    function during other initiating event scenarios. The effect on the 
    probability for a loss of RCP seal cooling due to losing CC cooling 
    to the RCP thermal barriers is negligible due to the high 
    reliability of the charging system to provide seal injection.
        The total effect of this DCP on core damage frequency (CDF) was 
    estimated by a sensitivity analysis combining both the change in the 
    reactor trip initiating event frequency and the increased failure 
    probability of RHR. It was evaluated that during implementation of 
    this DCP, CCHXs will be supplied from one SW header for 70 days (35 
    x 2=70), therefore, the increase in CDF previously evaluated in DCP-
    94-010 based on 140 days is conservative. This DCP does not affect 
    the containment systems and there would not be any significant 
    change in off-site dose since the containment heat removal portion 
    of the SW system is not affected and the increase in CDF is 
    insignificant. The small increase in CDF calculated for the repair 
    activities and the procedure developed to provide contingency 
    actions result in the conclusion that this work does not represent a 
    significant increase in core damage frequency.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to the allowed outage time only provide 
    operational flexibility needed to perform necessary repairs. During 
    the project, there will be a significant time period when all the 
    CCHXs are aligned to one SW loop. The possibility of an interruption 
    of SW supply to the heat exchangers during a DBA is eliminated by 
    defeating the closure of the 24-inch SW isolation MOVs [motor-
    operated valves] to the CCHXs on [an] SI/CDA [safety injection/
    containment depressurization actuation] signal. Both SW headers will 
    be available for equipment required for safe shutdown of the units 
    (i.e., RSHXs, charging pumps, and CR/ESGR [control room/emergency 
    switchgear room] chillers). The SW pipe repair activities and the 
    installation/removal of the SW cross-connect and temporary piping do 
    not create the possibility for a malfunction of equipment different 
    than previously evaluated. Results of the Johnston Pump NPSH [net 
    positive suction head] test proved to be satisfactory for the 
    anticipated SW pump flow rates under modes of station operation for 
    this project, therefore, the possibility for an accident of a 
    different type than was previously evaluated in the Safety Analysis 
    Report will not be created. Based on the above, implementation of 
    the restoration project and approval of the proposed Technical 
    Specifications changes will not introduce any new accident 
    initiators nor affect the performance of accident mitigation 
    systems.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to the schedule only provide operational 
    flexibility to perform the required SW pipe refurbishment. The 
    Technical Specifications continue to require the SW and CC systems 
    to remain functional during the period with a single SW supply to 
    the CCHXs. As stated in item (1) above, the SW system is fully 
    capable of performing its DBA function during the course of the pipe 
    refurbishment project with the proposed Technical Specification 
    changes in place. The effect of this pipe refurbishment project on 
    CC system reliability was estimated by a sensitivity analysis 
    combining both the change in the reactor trip initiating event 
    frequency and the increased failure probability of RHR resulting in 
    about a 1E-8 per year increase in CDF. Since this project will not 
    affect the containment systems, there would not be any significant 
    change in off-site dose, except that resulting directly from the 
    slight increase in CDF.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: F. Mark Reinhart (Acting)
    
    Notice of Issuance of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: September 10, 1996
        Brief description of amendments: The amendments extend the 
    automatic actuation logic channel functional test interval of the 
    Engineering Safety
    
    [[Page 6582]]
    
    Features Actuation System and the surveillances test interval of the 
    containment sump isolation valves from monthly to quarterly.
        Date of issuance: January 23, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 218 and 195
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52963) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated January 23, 1997 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: October 31, 1996
        Brief description of amendments: The amendments relocate the 
    requirements for seismic monitoring instrumentation from Technical 
    Specification (TS) 3/4.3.7.2, ``Seismic Monitoring Instrumentation'' to 
    licensee-controlled documents in accordance with Generic Letter 95-10, 
    ``Relocation of Selected Technical Specifications Requirements Related 
    to Instrumentation.'' The amendments also add a condition to the 
    operating licenses which approves the relocation of the TS requirements 
    to the UFSAR.
        Date of issuance: January 29, 1997 Effective date: Immediately, to 
    be implemented within 90 days.
        Amendment Nos.: 117, 102
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications and the license.
        Date of initial notice in Federal Register: December 18, 1996 (61 
    FR 66703) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 29, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley 
    Power Station, Unit No. 1, Shippingport, Pennsylvania
    
        Date of application for amendment: September 9, 1996, as 
    supplemented December 20, 1996
        Brief description of amendment: The amendment revises the Minimum 
    Channels Operable requirement of Item 4.c (Steam Line Isolation, 
    Containment Pressure Intermediate--High-High) of Technical 
    Specification (TS) Table 3.3-3 from 3 channels to 2 channels provided 
    the provisions of Action Statement 14 are followed. This change makes 
    this Beaver Valley Power Station, Unit No. 1 TS consistent with the 
    comparable Beaver Valley Power Station, Unit No. 2 TS. The amendment 
    also revises the minimum charging pump discharge pressure in TS 3/4.5.5 
    and associated Bases from 2311 psig to 2397 psig. This change ensures 
    that safety analysis assumptions for safety injection flow are met.
        Date of issuance: January 27, 1997
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment No: 201
        Facility Operating License No. DPR-66. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55032) The supplemental letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination or the original notice. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    January 27, 1997. No significant hazards consideration comments 
    received: No
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: August 15, 1996, and as 
    supplemented by letters dated October 28, November 15, 1996, and 
    January 7, 1997.
        Brief description of amendment: The amendment changes the Clinton 
    Power Station (CPS) Technical Specifications to incorporate the revised 
    Safety Limit Minimum Critical Power Ratio (SLMCPR) as calculated by 
    General Electric (GE) for CPS Cycle 7. The need to change the SLMCPR 
    resulted from the 10 CFR Part 21 condition reported by GE in their 
    letter to the NRC dated May 24, 1996.
        Date of issuance: January 22, 1997
        Effective date: January 22, 1997
        Amendment No.: 113
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47978). The licensee's letters of October 28, November 15, 1996, and 
    January 7, 1997, provided clarifying information and did not make 
    significant changes to the initial Federal Register notice. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated January 22, 1997. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: August 29, 1996
        Brief description of amendment: The amendment revises the Technical 
    Specifications to (1) modify the applicability requirements for certain 
    radiation monitors so that the radiation monitors are required to be 
    operable only when secondary containment integrity is required to be 
    operable; (2) delineate when secondary containment integrity is 
    required; (3) modify standby gas treatment operability requirements; 
    (4) make editorial corrections to clarify the configuration of the 
    radiation monitors; and (5) revise the associated Bases sections.
        Date of issuance: January 14, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 98
        Facility Operating License No. DPR-21: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 17, 1996 (61 FR 
    54242) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated January 14, 1997 No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: : Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385
    
    [[Page 6583]]
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: June 28, 1996, as supplemented 
    by letters dated November 4 and 5, and December 9, 1996
        Brief description of amendments: These amendments revise the 
    technical specifications to incorporate performance-based testing, in 
    accordance with 10 CFR Part 50, Appendix J, ``Primary Reactor 
    Containment Leakage Testing For Water-Cooled Power Reactors,'' Option 
    B. This option allows utilities to extend the frequencies of the Type A 
    Containment Leak Rate Test, and Type B and C Local Leak Rate Tests 
    based on the performance and design of the containment and components.
        Date of issuance: January 24, 1997
        Effective date: Both units, as of date of issuance and shall be 
    implemented within 30 days.
        Amendment Nos.: 118 and 81
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55038) The supplemental letters provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination or the original notice. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated Janaury 24, 1997. No significant hazards consideration 
    comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: May 20, 1996
        Brief description of amendments: These amendments revise Technical 
    Specifications (TS) Sections 3/4.4.9.2, 3/4.9.11.1, 3/4.9.11.2, and the 
    associated TS Bases 3/4.4.9 and 3/4.9.11, to more clearly describe that 
    the Residual Heat Removal (RHR) system Shutdown Cooling mode of 
    operation consists of four ``subsystems.'' These TS sections pertain to 
    plant operations during Operational Conditions (OPCONs) 4, ``Cold 
    Shutdown'' and 5, ``Refueling.'' In addition, the proposed TS change 
    would make administrative changes to TS Section 3/4.4.9.1 to ensure 
    consistency in terminology regarding the description of Shutdown 
    Cooling ``subsystems.'' The proposed TS changes are consistent with the 
    guidance delineated in the Improved TS (i.e., NUREG-1433, Revision 1, 
    ``Standard Technical Specifications General Electric Plants, BWR/4,'' 
    dated April 1995) which indicates that the RHR Shutdown Cooling mode of 
    operation is comprised of two loops and four subsystems (i.e., two 
    subsystems per loop).
        Date of issuance: January 28, 1997
        Effective date: As of date of issuance and shall be implemented 
    within 30 days.
        Amendment Nos.: 119 and 82
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55036) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 28, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
    
    Philadelphia Electric Company, Docket No. 50-353, Limerick 
    Generating Station, Unit 2, Montgomery County, Pennsylvania
    
        Date of application for amendment: August 5, 1996, as supplemented 
    December 4, 1996
        Brief description of amendment: The amendment revised TS Section 
    2.1 and its associated TS Bases to reflect the change in the Minimum 
    Critical Power Ratio Safety Limit due to the plant specific evaluation 
    performed by General Electric Company (GE), for Limerick Generating 
    Station, Unit 2, Cycle 4.
        Date of issuance: January 29, 1997
        Effective date: As of date of issuance and shall be implemented 
    within 30 days
        Amendment No.: 83
        Facility Operating License No. NPF-85. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 6, 1996 (61 FR 
    57491) The December 4, 1996, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination or the initial notice. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated January 29, 1997. No significant hazards consideration comments 
    received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: March 29, 1996, as supplemented 
    by letters dated December 5, 1996, and January 15, 1997
        Brief description of amendments: These amendments modify Technical 
    Specification (TS) Section 4.5.1.d.2.b to delete the requirement to 
    perform in-situ functional testing of the Automatic Depressurization 
    System (ADS) valves once every 24-months as part of start-up testing 
    activities.
        Date of issuance: January 29, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 120 and 84
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 6, 1996 (61 FR 
    57488) The December 5, 1996, and January 15, 1997, letters provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination nor the initial notice. 
    The Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated January 29, 1997. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: October 1, 1996
        Brief description of amendment: The amendment allows for a one-time 
    extension of the surveillance intervals for the containment isolation 
    valve seat leakage test, the isolation valve seal water test, the boron 
    injection tank leakage test, the containment spray nozzle test, and the 
    city water backup to the auxiliary boiler feed pump test.
        Date of issuance: January 28, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 172
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR
    
    [[Page 6584]]
    
    64393) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated January 28, 1997 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: October 1, 1996, supplemented 
    October 31, 1996
        Brief description of amendments: The amendments change Technical 
    Specifications 3/4.7.1.5, ``Main Steam Line Isolation Valves (MSIVs),'' 
    and 3/4.3.2, ``Engineered Safety Feature Actuation System 
    Instrumentation.'' The amendments accommodate entry into Modes 3 and 2 
    prior to performing MSIV closure time testing in Mode 2, allow 
    additional time for the repair and testing of inoperable MSIVs in 
    certain operating Modes, delete footnotes that are no longer 
    applicable, and change the low steam line pressure trip setpoint value 
    for safety injection, turbine trip and feedwater isolation to make it 
    consistent with the actual plant configuration.
        Date of issuance: January 17, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented prior to entry into Mode 3 from the current outage.
        Amendment Nos. 187 and 170
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55040) The supplemental letter changed the TSs to provide greater 
    consistency with requirements of NUREG-1431 ``Standard Technical 
    Specifications - Westinghouse Plants,'' Revision 1, and did not change 
    the initial proposed no significant hazards consideration determination 
    or the Federal Register notice. The Commission's related evaluation of 
    the amendments is contained in a Safety Evaluation dated January 17, 
    1997. No significant hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: October 24, 1996, as 
    supplemented December 23, 1996
        Brief description of amendments: The amendments changed Technical 
    Specification 3/4.7.1.2, ``Auxiliary Feedwater System.'' The changes 
    revised the 18-month surveillance performed on the system's pumps and 
    valves because testing of the turbine driven Auxiliary Feedwater pump 
    can only be performed in higher modes when there is sufficient 
    secondary steam pressure.
        Date of issuance: January 23, 1997
        Effective date: As of date of issuance, to be implemented within 30 
    days
        Amendment Nos. 188 and 171
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 19, 1996 (61 
    FR 58905) The December 23, 1996, letter proposed changes to TS 3/4.3.2 
    to provide consistency with those proposed in the October 24, 1996, 
    letter and therefore did not change the initial proposed no significant 
    hazards consideration determination and was within the scope of the 
    initial notice. The Commission's related evaluation of the amendments 
    is contained in a Safety Evaluation dated January 23, 1997. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: September 25, 1996
        Brief description of amendments: The amendments relocate the list 
    of containment isolation valves from the Technical Specifications to 
    the Salem Updated Final Safety Analysis Report and correct references. 
    Date of issuance: January 30, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented within 60 days.
        Amendment Nos. 189 and 172
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications and the License.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55039) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 30, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: January 31, 1996, as revised 
    November 26, 1996. The November 26, 1996, submittal withdrew the 
    proposed change to surveillance tests being performed at power.
        Brief description of amendments: These amendments will revise the 
    minimum emergency diesel generator day tank fuel oil volume.
        Date of issuance: January 17, 1997
        Effective date: January 17, 1997
        Amendment Nos.: 203 and 184
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7559) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 17, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: : The Alderman Library, 
    Special Collections Department, University of Virginia, 
    Charlottesville, Virginia 22903-2498.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: February 8, 1996, as 
    supplemented August 15, December 2 and December 19, 1996, and January 
    6, 1997
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) Section 15.3.10, ``Control Rod and Power 
    Distribution Limits,'' to improve the clarity of this section and add 
    surveillance requirements to Section 15.4.1, ``Operational Safety 
    Review.''
        Date of issuance: January 16, 1997
        Effective date: January 16, 1997, with full implementation within 
    45 days
        Amendment Nos.: Unit 1 - 171, Unit 2 - 175
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 13, 1996 (61 FR 
    10398) The August 15, December 2 and
    
    [[Page 6585]]
    
    December 19, 1996, and January 6, 1997, letters provided clarifying 
    information and updated TS pages that were within the scope of the 
    original application and did not change the NRC staff's initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated January 16, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point, Units 3 and 4, Dade County, Florida
    
        Date of amendment request: December 17, 1996
        Description of amendment request: The proposed amendments would 
    modify the Turkey Point Units 3 and 4 Technical Specifications to 
    change the Reactor Coolant Pump (RCP) flywheel surveillance 
    requirement. The proposed change will require RCP flywheel inspections 
    once every ten years.
        Date of publication of individual notice in Federal Register: 
    January 10, 1997 (62 FR 1476)
        Expiration date of individual notice: February 10, 1997
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of amendment request: December 13, 1996
        Description of amendment request: The proposed amendment would 
    approve transfer of Soyland Power Cooperative's 13.21% minority 
    ownership interest in the Clinton Power Station to Illinois Power 
    Company. This action would result in Illinois Power Company becoming 
    the sole owner of the Clinton Power Station.
        Date of publication of individual notice in Federal Register: 
    January 29, 1997 (62 FR 4337).
        Expiration date of individual notice: February 28, 1997
        Local Public Document Room location: : Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental
    
    [[Page 6586]]
    
    Assessment, as indicated. All of these items are available for public 
    inspection at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC, and at the local public 
    document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By March 14, 1997, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of application for amendments: January 13, 1997, as 
    resubmitted January 17, 1997, and supplemented January 22, 1997.
        Brief description of amendments: The proposed amendments would: 
    evaluate the Unreviewed Safety Question (USQ) associated with the 
    operation of Dresden, Units 2 and 3, with the recently discovered error 
    in the head loss across the Emergency Core Cooling System (ECCS) 
    suction strainers; change the Technical Specification (TS) values by 
    lowering the allowable water temperature in the suppression chamber and 
    ultimate heat sink; change the basis of the TS to allow credit for two 
    psig of containment pressure to compensate for a slight increase in the 
    amount of Net Positive Suction Head (NPSH) deficiency during the first 
    10 minutes following a design basis accident (DBA); and add a license 
    condition to allow the licensee to change the Updated Final Safety 
    Analysis Report to reflect the use of two psig of containment pressure 
    to compensate for the deficiency in NPSH during the first 10 minutes 
    following a DBA.
        Date of Issuance: January 28, 1997 Effective date: Immediately, to 
    be implemented within 30 days.
        Amendment Nos.: 152/147
        Facility Operating License Nos. DPR-19 and DPR-25. The amendments 
    revised the Technical Specifications and the Operating Licenses. Press 
    release issued requesting comments as to proposed no significant 
    hazards
    
    [[Page 6587]]
    
    consideration: Yes January 25, 1997 Joliet Herald News Comments 
    received: No. The Commission's related evaluation of the amendment, 
    finding of exigent circumstances, consultation with the State of 
    Illinois and determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated January 28, 1997.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450.
        NRC Project Director: Robert A. Capra
        Dated at Rockville, Maryland, this 5th day of February, 1997.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation
    [Doc. 97-3324 Filed 2-11-97; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
02/12/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X97-20212
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
6566-6587 (22 pages)
PDF File:
x97-20212.pdf