95-3520. Philadelphia Electric Co.; Limerick Generating Station, Units 1 and 2; Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 60, Number 29 (Monday, February 13, 1995)]
    [Notices]
    [Pages 8255-8259]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-3520]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-352 and 50-353]
    
    
    Philadelphia Electric Co.; Limerick Generating Station, Units 1 
    and 2; Environmental Assessment and Finding of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of an amendment to Facility Operating License No. 
    NPF-85, issued to Philadelphia Electric Company, (the licensee), for 
    operation of the Limerick Generating Station, Units 1 and 2, located in 
    Montgomery County, Pennsylvania.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        This Environmental Assessment has been prepared to address 
    potential environmental issues related to the licensee's application of 
    December 9, 1993, as supplemented July 5, September 9, October 19, 
    November 19, 1994, January 6, and January 23, 1995, to amend the 
    Limerick Generating [[Page 8256]] Station (LGS), Units 1 and 2 
    operating licenses. The proposed amendment would increase the licensed 
    thermal power level from 3293 Mwt to 3458 Mwt. This request is in 
    accordance with the generic boiling water reactor (BWR) power uprate 
    program established by the General Electric Company (GE) and approved 
    by U.S. Nuclear Regulatory Commission (NRC) staff in a letter of 
    September 30, 1991.
        The proposed action involves NRC issuance of a license amendment to 
    increase the authorized power level by changing the operating license, 
    including Appendix A of the license (Technical Specifications). No 
    change is needed to Appendix B of the license (Environmental Protection 
    Plan--Non-radiological).
    
    The Need for the Proposed Action
    
        The proposed action is needed to permit an increase in the licensed 
    core thermal power from 3293 Mwt to 3458 Mwt and provide the licensee 
    with the flexibility to increase the potential electrical output of 
    LGS, Units 1 and 2, providing additional electrical power to service 
    domestic and commercial areas.
    
    Environmental Impacts of the Proposed Action
    
        The ``Final Environmental Statement (FES) Related to Operation of 
    Limerick Generating Station, Units 1 and 2'' was issued April 1984 
    (NUREG-0974). The licensee submitted GE Topical Report, NEDC-32225P, 
    ``Power Rerate Safety Analysis Report for Limerick Generating Station, 
    Units 1 and 2,'' Class III, dated September 1993, as Attachment 3 to 
    the December 9, 1993 submittal. NEDC-32225P contains the safety 
    analysis prepared by GE to support this license change request and the 
    implementation of power uprate at LGS, Units 1 and 2. The analyses and 
    evaluations supporting these proposed changes were completed using the 
    guidelines in GE Topical Report NEDC-31897P-A, ``Generic Guidelines for 
    General Electric Boiling Water Reactor Power Uprate,'' Class 3, dated 
    May 1992, and NEDC-31948P, ``Generic Evaluations of General Electric 
    Boiling Water Reactor Power Uprate,'' Class III, dated July 1991. The 
    NRC reviewed and approved GE Topical Reports NEDC-31897P-A and NEPC-
    31948P in a September 30, 1991, letter and in a letter from W. Russell, 
    NRC, to P. Marriotte, GE, dated July 31, 1992.
        The licensee provided information regarding the nonradiological and 
    radiological environmental effects of the proposed action in the 
    December 9, 1993 application and supplemental information in the 
    January 6, and January 23, 1995 submittal. The staff has reviewed the 
    potential radiological and non-radiological effects of the proposed 
    action on the environment as described below.
    
    Non-Radiological Environmental Assessment
    
        Power uprate will not change the method of generating electricity 
    nor the method of handling any influents from nor effluents to the 
    environment. Therefore, no new or different types of environmental 
    impacts are expected.
        The staff reviewed the nonradiological impact of operation at 
    uprated power levels on influents from the Perkiomen Creek, Schuylkill 
    and Delaware Rivers and effluents to the Schuylkill River. LGS, Units 1 
    and 2 each have a closed-loop circulating water system and cooling 
    tower for dissipating heat from the main turbine condensers. The 
    cooling towers are operated in accordance with the requirements of 
    National Pollution Discharge Elimination System (NPDES) Permit No. 
    PA0051926. The current permit was renewed on December 12, 1994 and is 
    effective through December 31, 1999. The only increase in LGS water 
    intake due to operation at power uprate conditions is due to increased 
    evaporation in the hyperbolic natural draft cooling towers. In the 
    January 6, 1995 letter, the licensee indicated that the existing 
    consumptive flow will conservatively increase from 38,059,065 to 
    40,723,200 gallons per day (total for both units), depending on 
    atmospheric conditions. The velocity of the intake water will increase 
    less than 7 percent. Makeup is drawn from the Schuylkill River, 
    Perkiomen Creek, or the Delaware River, depending on flow and 
    temperature. When makeup is drawn from the Delaware River through the 
    Point Pleasant Pumping Station via the Bradshaw Station, 3 percent 
    additional evaporative losses must be considered. The increase makeup 
    flow (including evaporative losses), is within the existing water 
    diversion consumptive use limit of 42,000,000 gallons per day specified 
    in the original permitting evaluations.
        Makeup water requirements for systems and components other than the 
    cooling towers are not expected to change due to operation at uprated 
    power levels. The licensee indicated that the only potential change is 
    due to increased reactor operating pressure which could slightly 
    increase leakage through valve packing. System leakage, however, is 
    processed through the liquid radwaste system and returned to the 
    condensate storage tank for reuse. Based on the above considerations, 
    the staff concluded that the effect of makeup requirements at uprated 
    power levels on the environment is not significant.
        The licensee does not expect any increase in the cooling tower 
    blowdown due to the physical limitation in the blowdown system. 
    Likewise, the licensee does not expect any increase in the blowdown 
    discharge velocity. However, the licensee indicated that the blowdown 
    discharge temperature will increase less than 0.1 deg.F. This 
    temperature rise will have an insignificant effect on the thermal 
    plume. This increase is within the NPDES permit limit.
        An increase in cooling tower drift is not anticipated for operation 
    at uprated conditions. Drift is a function of physical geometry, water 
    flow, and wind conditions, none of which are changed by power uprate. 
    Therefore, the licensee has indicated that the original evaluation of 
    impacts to the terrestrial environment is not altered.
        The only changes to the cooling tower water chemistry are due to 
    increased evaporation from the towers. Concentrations of dissolved and 
    suspended solids in the blowdown will increase approximately less than 
    7 percent, which is within NPDES permit limits. The licensee stated 
    that the use of biocides and corrosion inhibitors in the circulating 
    water system may change as a result of operation at uprated power 
    levels. However, the licensee stated that change in chemical usage 
    would not impact existing NPDES permit limitations.
        Nonradiological effluent discharges from other systems were also 
    considered. Nonradiological effluent limits for such systems as yard 
    drains, sewage treatment plant, and laundry drains are established in 
    the NPDES permit. Discharges from these systems are not expected to 
    change significantly, if at all, because operation at uprated power 
    levels is governed by the limits in the NPDES permit. Thus, the impact 
    on the environment from these systems as a result of operation at 
    uprated power levels is not significant.
        Operation at uprated power levels will not result in increased 
    noise generation from the majority of plant equipment. Some of this 
    equipment, such as the main turbine and generator will operate at the 
    same speed and thus will not contribute to increased offsite noise. 
    Other major plant equipment is located within plant structures and will 
    not lead to increased offsite noise levels. The main station 
    transformers will operate at an increased kilovolt-ampere level which 
    will cause an insignificant increase in the overall noise level. The 
    [[Page 8257]] makeup pumps, which are indoors, will operate at the same 
    level, however, in some cases cycling on slightly more frequently. The 
    pumps at the Bradshaw Station are variable speed and, when used, will 
    operate at a slightly higher speed. The pumps are indoors; therefore, 
    the outside noise level increase will be insignificant.
        The licensee has stated that there are no changes required to the 
    LGS Environmental Protection Plan as a result of operation at uprated 
    power levels. Specifically the licensee stated:
    
        Other non-radiological environmental impacts of the proposed 
    power rerate were reviewed based on the information submitted in the 
    Environmental Report, Operating License Stage, the NRC Final 
    Environmental Statement (FES), Operating License Appendix B (i.e., 
    Environmental Protection Plan), the requirements of the applicable 
    NPDES permits, which include the outfall limits, and the Delaware 
    River Basin Commission Water Use permit. We have concluded the 
    proposed power rerate will have insignificant impacts on the non-
    radiological elements of concern and the plant will be operated in 
    an environmentally acceptable manner as established by the FES. 
    Existing Federal, State and Local regulatory permits presently in 
    effect will accommodate power rerate without modification.
    
        The FES described the impact of plant operation on fogging in the 
    vicinity of the facility. The FES discussed that the increase in 
    fogging due to plant operation was expected to blend in with the 
    natural fog and be indistinguishable. The staff expects that operation 
    of the plant at uprated power levels will result in only a minimal 
    increase in fogging over that discussed in the FES. Thus, the impact of 
    plant operation on local fogging, including operation at uprated power, 
    remains insignificant.
    
    Radiological Environmental Assessment
    
        The licensee evaluated the impact of the proposed amendment to show 
    that the applicable regulatory acceptance criteria continue to be 
    satisfied for the uprated power conditions. In conducting this 
    evaluation, the licensee considered the effect of the higher power 
    level on source terms, onsite and offsite doses, and control room 
    habitability during both normal operation and accident conditions. The 
    licensee provided information regarding the radiological environmental 
    effects of the proposed action in NEDC-32225P and supplemental 
    information in the January 6, 1995 submittal. In Sections 8.1 and 8.2 
    of NEDC-32225P, the licensee discussed the potential effect of power 
    rerate on liquid and gaseous radioactive waste systems. Sections 8.3 
    and 8.4 discussed the potential effect of power uprate on radiation 
    sources in the reactor coolant resulted from coolant activation 
    products, activated corrosion products and fission products. Section 
    8.5 of the Topical Report discussed the radiation levels during normal 
    operation, normal post-operation, post-accident, and offsite doses 
    during normal operation. Finally, Section 9.2 of NEDC-32225P presented 
    the results of calculated whole body and thyroid doses at the uprated 
    power and current authorized power conditions at the exclusion area 
    boundary and the low population zone that might result from the 
    postulated design basis radiological accidents [i.e., loss-of-coolant-
    accident (LOCA), main steam line break accident (MSLBA) outside 
    containment, fuel handling accident (FHA) and control rod drop accident 
    (CRDA)].
        In Section 8.1 of NEDC-32225P, the licensee stated that there will 
    be only a slight increase in the liquid radwaste collection as a result 
    of operation at higher power levels. The liquid waste system collects, 
    monitors, processes, stores, and returns processed radioactive waste to 
    the plant for reuse or for discharge. The largest contributor to the 
    liquid waste results from the backwash of the condensate demineralizers 
    and deepbeds. The rate of loading on the demineralizers increases, 
    resulting in the average time between backwash precoat being reduced 
    slightly; this reduction does not affect plant safety. Similarly, the 
    reactor water cleanup (RWCU) filter/demineralizers will require 
    slightly more frequent backwashes due to slightly higher levels of 
    activation and fission products. The power uprate will increase the 
    flow rate through the condensate demineralizers, with a subsequent 
    reduction in the average time between backwashing. Additionally, 
    neither the floor drain collector subsystem nor the waste collector 
    subsystem is expected to experience a significant increase in the total 
    volume of liquid waste due to operation at the uprated level.
        The licensee stated that while the activated corrosion products in 
    liquid wastes are expected to increase proportionally to the square of 
    the power increase, the total volume of processed waste is not expected 
    to increase appreciably. Based on its analyses of the liquid radwaste 
    system, the licensee has concluded the requirements of 10 CFR part 20 
    and 10 CFR part 50, appendix I, will be met. Based on the above 
    considerations, the staff concluded that the power uprate will have no 
    significant adverse effects on liquid effluents.
        The gaseous waste management systems collect, control, process, 
    store and dispose of gaseous radioactive waste generated during normal 
    operation and abnormal operational occurrences. These systems include 
    the standby gas treatment system (SGTS), off-gas recombiner system, the 
    ambient temperature charcoal treatment system, and various building 
    ventilation systems. Various devices and processes, such as radiation 
    monitors, filters, isolation dampers, and fans, are used to control 
    airborne radioactive gases. The licensee states that the activity of 
    airborne effluents released through building vents is not expected to 
    increase significantly with power uprate and the systems are designed 
    to meet the requirements of 10 CFR part 20 and 10 CFR part 50, appendix 
    I.
        In its power uprate submittal, the licensee has stated that the 
    greatest contributor of radioactive gases is the noncondensible 
    radioactive gases from the main condenser, including activation gases 
    (principally N-16, O-19, and N-13) and radioactive noble gas parents. 
    The increase in production of these gases is expected to be 
    approximately proportional to the core power increase. These 
    noncondensible radioactive gases, along with nonradioactive air due to 
    inleakage to the condenser, are continuously removed from the main 
    condensers by the stream jet air ejectors (SJAE). The SJAEs discharge 
    into the offgas system. The flow of these gases into the offgas system 
    is included with the flow of H2 and 02 to the recombiner, 
    which will also increase linearly with core power. Radioactive gases 
    and H2 and 02 pass from the recombiner through a holdup pipe, 
    cooler condenser, adsorber bed, and high-efficiency particulate air 
    (HEPA) filters and exit the facility through the north stack. Gaseous 
    activity effluent release rates are monitored down stream of the 
    adsorber bed and alarms are provided in the control room. The licensee 
    has stated that the operational increases in hydrogen, oxygen, and 
    noble gases due to uprate are not significant when compared to the 
    current total system flow which also includes air from condenser 
    inleakage and steam flows from the air ejector.
        The design basis for the offgas system is for activity release 
    rates of 100,000 microcuries per second based on a mixture of 
    activation and fission product gases and fuel leakage and a 30-minute 
    holdup time. The system is designed to meet the requirements of 10 CFR 
    part 20 and 10 CFR part 50, appendix I. Performance of the system at 
    uprated power levels is expected to remain within the system design 
    basis and, thus, to continue to meet the [[Page 8258]] requirements of 
    10 CFR part 20 and 10 CFR part 50, appendix I.
        The contribution of gases to the gaseous waste management system 
    from building ventilation system is not expected to increase 
    significantly with power uprate because (1) the amount of fission 
    products released into the reactor coolant depends on the number of 
    nature of the fuel rod defects and is not dependent on reactor power, 
    and (2) the concentration of coolant activation products is expected to 
    remain unchanged since the linear increase in the production of these 
    products will be offset by the linear increase in steaming rate.
        Based on its review of the gaseous waste management system, the 
    staff concluded that there will not be a significant adverse effect on 
    airborne effluents as a result of the power rerate.
        The licensee has evaluated the effects of the power uprate on in-
    plant radiation levels in the LGS facility during normal and abnormal 
    operation as well as from postulated accident conditions. The licensee 
    has concluded that radiation levels from both normal and accident 
    conditions may increase slightly. However, because many areas of the 
    plant were designed for higher than expected radiation sources, the 
    small increase in radiation levels expected due to power uprate will 
    not affect radiation zoning or shielding in the plant.
        During periods of normal and post-operation conditions, individual 
    worker exposures will be maintained within acceptable limits by the 
    existing, as low as is reasonably achievable (ALARA) program, which 
    controls access to radiation areas. Procedure controls compensate for 
    slightly increased radiation levels.
        The offsite doses associated with normal operation are not 
    significantly affected by operation at the uprated power level, and are 
    expected to remain below the limits of 10 CFR part 20 and 10 CFR part 
    50, appendix I.
        The main control room (MCR) habitability was evaluated. Post-
    accident MCR and technical support center doses were confirmed by the 
    licensee to be within the limits of General Design Criterion (GDC) 19 
    or 10 CFR part 50, appendix A.
        The increase in LOCA radiological consequences due to power uprate 
    was analyzed by the licensees. The resultant offsite doses were found 
    to be within guidelines of 10 CFR part 100. The events evaluated for 
    uprate were the LOCA, the MSLBA, the FHA, and the CRDA. The whole body 
    and thyroid doses were calculated for the exclusion area boundary 
    (EAB), low population zone (LPZ), and the control room. The plant-
    specific results for power uprate remain well below established 
    regulatory limits. The doses resulting from the accidents analyzed are 
    compared below with the applicable dose limits.
    
    ------------------------------------------------------------------------
                                                 LOCA radiological          
                                                   consequences             
                                               --------------------         
                                                  UFSAR                     
                     Location                     dose      Dose      Limit 
                                                  (rem)    (rem) @          
                                                  @3458     3527            
                                                   MWt     MWt\1\           
    ------------------------------------------------------------------------
    Exclusion area:                                                         
      Whole body dose.........................     0.67     0.68          25
      Thyroid dose............................     0.15     0.15         300
    Low population zone:                                                    
      Whole body dose.........................     1.7      1.7           25
      Thyroid dose............................     0.04     0.04         300
    Main control room:                                                      
      Whole body dose.........................     4.6      4.7            5
      Thyroid dose............................    14.0     14.3           30
      Beta....................................     7.6      7.8           30
                                                                            
    ------------------------------------------------------------------------
                          FHA Radiological Consequences                     
                                                                            
    ------------------------------------------------------------------------
    Exclusion area:                                                         
      Whole body dose.........................     0.7      0.7            6
      Thyroid dose............................     0.95     0.98          75
                                                                            
                                                                            
    Low population zone:                                                    
      Whole body dose.........................     0.099    0.102          6
      Thyroid dose............................     0.13     0.135         75
                                                                            
    ------------------------------------------------------------------------
                         CRDA Radiological Consequences                     
                                                                            
    ------------------------------------------------------------------------
    Exclusion area:                                                         
      Whole body dose.........................     0.04     0.042          6
      Thyroid dose............................     0.32     0.3           75
    Low population zone:                                                    
      Whole body dose.........................     0.014    0.0148         6
      Thyroid dose............................     0.62     0.63          75
    ------------------------------------------------------------------------
    \1\This number represents 102% of the power uprate level. Doses based on
      102% are consistent with Regulatory Guide 1.49, Revision 1 guidance   
      and are provided to allow for possible instrument errors in           
      determining the power level.                                          
    
        Based on a review of the licensee's major assumptions and 
    methodology used in their reconstituted dose calculations and the 
    staff's original safety evaluation, the staff concluded that the 
    offsite radiological consequences and control room operator doses at 
    uprated power levels still remain below 10 CFR part 100 dose reference 
    values and GDC 19 dose limits. Therefore, the staff concludes that no 
    significant adverse effect on radiation levels will result onsite or 
    offsite from the planned power uprate.
        It is expected that the increased energy requirements associated 
    with operation at uprated power will require an increase in the reload 
    fuel enrichment and will result in increased burnup. The NRC previously 
    evaluated the environmental impacts associated with burnup values of up 
    to 60,000 MWd/MT with fuel enrichments up to 5 percent 235U 
    (published in the Federal Register, 53 FR 6040 dated February 29, 
    1988). The staff concluded that the environmental impacts associated 
    with Table S-3 of 10 CFR 51.51, Uranium Fuel Cycle Environmental Data, 
    and Table S-4 of 10 CFR 51.52, Environmental Impact of Transportation 
    of Fuel and Waste, are conservative and bound the corresponding impacts 
    for burnup levels of up to 60,000 MWd/MtU and 235U enrichments up 
    to 5 percent by weight. In the January 23, 1995 submittal, the licensee 
    indicated that while fuel burnup and enrichment levels may increase as 
    a result of operation at uprated power, the burnup and enrichment will 
    remain within the 5 percent enrichment and 60,000 MWd/MT value 
    previously evaluated by the staff. Based on the above cited 
    environmental assessment and the licensee's statements regarding 
    expected burnup and enrichment values, the staff concludes that the 
    environmental effects of increased fuel cycle and transportation 
    activity as a result of operation at uprated power levels are not 
    significant. [[Page 8259]] 
        The Commission has completed its evaluation of the proposed action 
    and concludes that the NRC's FES is valid for operation at the proposed 
    uprated power conditions for LGS, Units 1 and 2. The staff also 
    concluded that the plant operating parameters impacted by the proposed 
    uprate would remain within the bounding conditions on which the 
    conclusions of the FES are based.
        The change will not increase the probability or consequences of 
    accidents, no changes are being made in the types of any effluents that 
    may be released offsite, and there is no significant increase in the 
    allowable individual or cumulative occupational radiation exposure.
        The NRC staff finds the radiological and nonradiological 
    environmental impacts associated with the proposed small increase in 
    power are very small and do not change the conclusion in the FES that 
    the operation of LGS, Units 1 and 2, would cause no significant adverse 
    impact upon the quality of the human environment.
        Accordingly, the Commission concludes that there are no significant 
    radiological environmental impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there is no measurable 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated.
        The principal alternative to the action would be to deny the 
    request. Such action would not significantly reduce the environmental 
    impact of plant operation but would restrict operation of LGS, Units 1 
    and 2 to the currently licensed power level and prevent the facility 
    from generating approximately 60 MWe (165 MWt) additional that is 
    obtainable from the existing plant design.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the ``Final Environmental Statement related to 
    the operation of Limerick Generating Station, Units 1 and 2,'' dated 
    April 1984.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, the staff consulted with the 
    Bureau of Radiation Protection, Pennsylvania Department of 
    Environmental Resources, regarding the environmental impact of the 
    proposed action. The State official had no comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated December 9, 1993, as supplemented by letters 
    dated July 5, September 9, October 19, and November 19, 1994, and 
    January 6, and January 23, 1995, which are available for public 
    inspection at the Commission's Public Document Room, The Gelman 
    Building, 2120 L Street, NW., Washington, DC, and at the local public 
    document room located at the Pottstown Public Library, 500 High Street, 
    Pottstown, PA 19464.
    
        Dated at Rockville, Maryland, this 7th day of February 1995.
    
        For the Nuclear Regulatory Commission.
    Chester Poslusny,
    Acting Director, Project Directorate I-2, Division of Reactor 
    Projects--I/II, Office of Nuclear Reactor Regulation.
    [FR Doc. 95-3520 Filed 2-10-95; 8:45 am]
    BILLING CODE 7590-01-M
    
    

Document Information

Published:
02/13/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-3520
Pages:
8255-8259 (5 pages)
Docket Numbers:
Docket Nos. 50-352 and 50-353
PDF File:
95-3520.pdf