95-3629. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations; Biweekly Notice  

  • [Federal Register Volume 60, Number 31 (Wednesday, February 15, 1995)]
    [Notices]
    [Pages 8741-8766]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-3629]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations; Biweekly Notice
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from January 20, 1995, through February 3, 1995. 
    The last biweekly notice was published on February 1, 1995 (60 FR 
    6296).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By March 17, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the [[Page 8742]] bases of the contention and a 
    concise statement of the alleged facts or expert opinion which support 
    the contention and on which the petitioner intends to rely in proving 
    the contention at the hearing. The petitioner must also provide 
    references to those specific sources and documents of which the 
    petitioner is aware and on which the petitioner intends to rely to 
    establish those facts or expert opinion. Petitioner must provide 
    sufficient information to show that a genuine dispute exists with the 
    applicant on a material issue of law or fact. Contentions shall be 
    limited to matters within the scope of the amendment under 
    consideration. The contention must be one which, if proven, would 
    entitle the petitioner to relief. A petitioner who fails to file such a 
    supplement which satisfies these requirements with respect to at least 
    one contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: January 19, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Surveillance Requirement 4.0.3 and 
    its associated bases to provide for a delay period of up to 24 hours in 
    which to perform a surveillance which has been discovered not to have 
    been performed within its specified frequency. This change would adopt 
    the requirements of NUREG-1431, ``Standard Technical Specifications, 
    Westinghouse Plants.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        The proposed change will reduce the requirement to unnecessarily 
    manipulate and challenge plant systems and equipment. The most probable 
    result of performing a surveillance during the delay period will be to 
    verify its conformance with Technical Specification requirements. Since 
    this change does not affect plant design, operation, or the manner in 
    which testing is performed, the consequences of accident scenarios 
    postulated in the Final Safety Analysis Report will not increase. 
    Therefore, there would be no increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed change does not introduce any new equipment, nor does 
    it require existing systems to perform a different type of function 
    than they are currently designed to perform. Therefore, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed amendment does not involve a significant reduction 
    in the margin of safety.
        The margin of safety is neither described or prescribed for this 
    specification. The proposed change simply provides additional time to 
    perform a surveillance and verify that the operability of equipment is 
    in conformance with the Technical Specification requirements. 
    Therefore, the proposed change does not involve a significant reduction 
    in [the] margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
        NRC Project Director: William H. Bateman.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: December 23, 1994.
        Description of amendment request: The proposed amendments would 
    increase the allowable enrichment of new fuel stored in the new fuel 
    storage vault (NFSV), revise the enrichment description of fuel in the 
    reactor core, and include references to documents previously approved 
    by the staff in the [[Page 8743]] Technical Specifications that provide 
    analytical methods used to determine core operating limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A.1. The proposed change does not involve a significant increase in 
    the probability of occurrence or consequences of any accident 
    previously evaluated.
        The Updated Final Safety Analysis Report (UFSAR) does not consider 
    any accidents involving the NFSV. The Fuel Handling Accidents that are 
    analyzed (Section 15.7.4) include dropping of a spent fuel assembly 
    onto the spent fuel pool floor and breaking of all fuel rods, and 
    dropping of a fuel assembly inside containment onto the top of the 
    core.
        The proposed change to increase the NFSV fuel enrichment limit from 
    4.0 to 4.65 weight percent U-235 does not affect any of the initiators 
    or precursors of any accident previously evaluated. The proposed change 
    will not increase the likelihood that a transient initiating event will 
    occur because transients are initiated by equipment malfunction and/or 
    catastrophic system failure. Since the proposed change does not involve 
    the introduction of new or redesigned plant equipment, failure 
    mechanisms are not affected. As a result, the probability of occurrence 
    of accidents previously evaluated is not significantly increased.
        A new criticality analysis for the proposed change to increase the 
    NFSV fuel enrichment limit from 4.0 to 4.65 weight percent U-235 was 
    performed for the NFSV. It was determined that even in worst case 
    conditions the acceptance criteria was met since the maximum Keff 
    was determined to be well below the 0.95 limit with a 95/95 
    probability/confidence level. The consequences of any accident, 
    including a fuel handling accident involving the NFSV, are not 
    significantly increased.
        A.2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        The proposed change to the Technical Specifications does not 
    involve the addition of any new or different types of safety related 
    equipment, nor does it involve the operation of equipment required for 
    safe operation of the facility in a manner different from those 
    addressed in the safety analysis. No safety related equipment or 
    function will be altered as a result of the proposed changes. Also, the 
    procedures governing normal plant operation and recovery from an 
    accident are not changed by the proposed Technical Specification 
    changes. Since no new failure modes or mechanisms are added by the 
    proposed changes, the possibility of a new or different kind of 
    accident is not created.
        A.3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Plant safety margins are established through LCOs, limiting safety 
    system settings, and safety limits specified in the Technical 
    Specifications. There will be no changes to either the physical design 
    of the plant or to any of these settings and limits as a result of 
    increasing the NFSV fuel enrichment limit. The change does not involve 
    a significant increase in the probability of occurrence or consequences 
    of any accident previously evaluated or create the possibility of a new 
    or different kind of accident from any previously analyzed. 
    Additionally, the revised criticality analysis demonstrates that the 
    maximum Keff under all postulated conditions remains below the 
    acceptance value of 0.95. Therefore, the change will not result in a 
    significant reduction in a margin of safety.
        B.1. The proposed change does not involve a significant increase in 
    the probability of occurrence or consequences of any accident 
    previously evaluated.
        The proposed change to increase the reactor core fuel enrichment 
    range discussed in the Design Features section of Technical 
    Specifications from ``between 2.2 to 4.0'' to ``up to 4.65'' weight 
    percent U-235 is administrative in nature and does not affect any of 
    the initiators or precursors of any accident previously evaluated. The 
    proposed change will not increase the likelihood that a transient 
    initiating event will occur because transients are initiated by 
    equipment malfunction and/or catastrophic system failure. Since the 
    proposed change does not involve the introduction of new or redesigned 
    plant equipment, failure mechanisms are not affected. As a result, the 
    probability of occurrence of accidents previously evaluated is not 
    significantly increased.
        The fuel enrichment limit of each core is determined by the core 
    specific design and is determined to be acceptable with respect to the 
    accident analysis by the reload analysis and is not impacted by the 
    value specified in the description in the Design Features section of 
    Technical Specifications. This value is only provided as the highest 
    expected core fuel enrichment in the Design Features section discussion 
    of the reactor core. This change is administrative in nature and does 
    not affect the consequences of any accident previously evaluated.
        B.2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        The proposed change in the reactor core fuel enrichment description 
    contained in the Design Features section of Technical Specifications 
    does not involve the addition of any new or different types of safety 
    related equipment, nor does it involve the operation of equipment 
    required for safe operation of the facility in a manner different from 
    those addressed in the safety analysis. No safety related equipment or 
    function will be altered as a result of the proposed change. Also, the 
    procedures governing normal plant operation and recovery from an 
    accident are not changed by the proposed Technical Specification 
    change. Since no new failure modes or mechanisms are added by the 
    proposed change, the possibility of a new or different kind of accident 
    is not created.
        B.3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Plant safety margins are established through LCOs, limiting safety 
    system settings, and safety limits specified in the Technical 
    Specifications. There will be no changes to either the physical design 
    of the plant or to any of these settings and limits as a result of 
    increasing reactor core fuel enrichment value given in the Design 
    Features section of Technical Specifications. The change does not 
    involve a significant increase in the probability of occurrence or 
    consequences of any accident previously evaluated or create the 
    possibility of a new or different kind of accident from any previously 
    analyzed.
        Based on the above discussion, the ability to safely shutdown the 
    operating unit and mitigate the consequences of all accidents 
    previously evaluated will be maintained. Therefore, the margin of 
    safety is not significantly affected.
        C.1. The proposed change does not involve a significant increase in 
    the probability of occurrence or consequences of any accident 
    previously evaluated.
        The proposed change to add three documents to the list of documents 
    that provide the analytical methods to determine core operating limits 
    is administrative in nature and does not affect any of the initiators 
    or precursors of any accident previously evaluated. The proposed change 
    will not increase the likelihood that a transient initiating event will 
    occur because transients are initiated by equipment malfunction 
    [[Page 8744]] and/or catastrophic system failure. Since the proposed 
    change does not involve the introduction of new or redesigned plant 
    equipment, failure mechanisms are not affected.
        The documents have been previously reviewed and approved by the NRC 
    and it was determined that they provide an acceptable means to 
    determine core operating limits. As a result, the probability of 
    occurrence of accidents previously evaluated is not significantly 
    increased. Since the documents provide NRC approved methodologies for 
    determining core operating limits, the addition of the documents to 
    Technical Specifications or use of the documents to determine core 
    operating limits will not significantly increase the consequences of 
    any accident previously evaluated.
        C.2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        The proposed change to add three documents to the list of documents 
    that provide the analytical methods to determine core operating limits 
    is administrative in nature and does not involve the addition of any 
    new or different types of safety related equipment, nor does it involve 
    the operation of equipment required for safe operation of the facility 
    in a manner different from those addressed in the safety analysis. No 
    safety related equipment or function will be altered as a result of the 
    proposed changes. Also, the procedures governing normal plant operation 
    and recovery from an accident are not changed by the proposed Technical 
    Specification changes. Since no new failure modes or mechanisms are 
    added by the proposed changes, the possibility of a new or different 
    kind of accident is not created.
        C.3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Plant safety margins are established through LCOs, limiting safety 
    system settings, and safety limits specified in the Technical 
    Specifications. There will be no changes to either the physical design 
    of the plant or to any of these settings and limits as a result of 
    adding references to the new documents. The ability to mitigate the 
    consequences of all accidents previously evaluated will be maintained. 
    Therefore, the margin of safety is not significantly affected.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: Robert A. Capra.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York Date 
    of amendment request: September 19, 1994.
    
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Section 4.4.A.3 to reference the 
    testing frequency requirements of 10 CFR Part 50, Appendix J, and to 
    state that NRC approved exemptions to the applicable regulatory 
    requirements are permitted. This proposed administrative revision 
    simply deletes the paraphrased language and directly references 
    Appendix J.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    Criterion 1--Does Not Involve a Significant Increase in the Probability 
    or Consequences of an Accident Previously Evaluated
        The proposed change will provide a one-time exemption from the 10 
    CFR [Part] 50, Appendix J Section III.D.1.(a) leak rate test schedule 
    requirement. This change will allow for a one-time test interval for 
    Type A Integrated Leak Rate Tests (ILRTs) of approximately 70 months.
        Leak rate testing is not an initiating event in any accident, 
    therefore this proposed change does not involve a significant increase 
    in the probability of a previously evaluated accident.
        Type A tests are capable of detecting both local leak paths and 
    gross containment failure paths. The history at IP-2 [Indian Point 2] 
    demonstrates that Type B and C Local Leak Rate Tests (LLRTs) have 
    consistently detected any excessive local leakages.
        Administrative controls govern the maintenance and testing of 
    containment penetrations such that the probability of excessive 
    penetration leakage due to improper maintenance or valve misalignment 
    is very low. Following maintenance on any containment penetration, an 
    LLRT is performed to ensure acceptable leakage levels, following any 
    LLRT on a containment isolation valve, an independent valve alignment 
    check is performed. Therefore, Type A testing is not necessary to 
    ensure acceptable leakage rates through containment penetrations.
        While Type A testing is not necessary to ensure acceptable leakage 
    rates through containment penetrations, Type A testing is necessary to 
    demonstrate that there are no gross containment failures. Structural 
    failure of the containment is considered to be a very unlikely event, 
    and in fact, since IP-2 has been in operation it has never failed a 
    Type A ILRT. Therefore, a one-time exemption increasing the interval 
    for performing an ILRT should not result in a significant decrease in 
    the confidence in the leak tightness of the containment structure.
        The proposed change also revises Technical Specification 4.4.A.3 to 
    reference the testing frequency requirements of 10 CFR [Part] 50, 
    Appendix J, and to state that NRC approved exemptions to the applicable 
    regulatory requirements are permitted. The current language of TS 
    4.4.A.3 paraphrases the requirements of Section III.D.1.(a) of Appendix 
    J. The proposed administrative revision simply deletes the paraphrased 
    language and directly references Appendix J. No new requirements are 
    added, nor are any existing requirements deleted. Any specific changes 
    to the requirements of Section III.D.1.(a) will require a submittal 
    from Consolidated Edison under 10 CFR 50.12 and subsequent review and 
    approval by the NRC prior to implementation. The proposed change is 
    stated generically to avoid the need for further TS changes if 
    different exemptions are approved in the future.
        The proposed change, in itself, does not affect reactor operations 
    or accident analysis and has no radiological consequences. The change 
    provides clarification so that future Technical Specifications changes 
    will not be necessary to correspond to applicable NRC approved 
    exemptions from the requirements of Appendix J.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of any accident previously 
    evaluated.
    Criterion 2--Does Not Create the Possibility of a New or Different Kind 
    of Accident from any Previously Evaluated.
        The proposed exemption request does not affect normal plant 
    operations or configuration, nor does it affect leak rate test methods. 
    The proposed change allows a one-time test interval of 
    [[Page 8745]] approximately 70 months for the ILRT. Given the test 
    history of IP-2 of no Type A test failures during plant lifetime, the 
    relaxation in schedule should not significantly decrease the confidence 
    in the leak tightness of the containment.
        The proposed Technical Specification amendment provides 
    clarification to a specification that paraphrases a codified 
    requirement.
        Since the proposed change would not change the design, 
    configuration or method of operation of the plant, it would not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated.
    Criterion 3--Does Not Involve a Significant Reduction in the Margin of 
    Safety.
        The purpose of the existing schedule for ILRTs is to ensure that 
    the release of radioactive materials will be restricted to those leak 
    paths and leak rates assumed in accident analyses. The relaxed schedule 
    for ILRTs does not allow for relaxation of Type B and C LLRTs. 
    Therefore, methods for detecting local containment leak paths and leak 
    rates are unaffected by this proposed change. Given that the test 
    history for ILRTs shows no failure during plant life, a one-time 
    increase of the test interval does not lead to a significant 
    probability of creating a new leakage path or increased leakage rates, 
    and the margin of safety inherent in existing accident analyses is 
    maintained.
        The proposed Technical Specification change is administrative and 
    clarifies the relationship between the requirements of TS 4.4.A.3, 
    Appendix J and any approved exemptions to Appendix J. It does not, in 
    itself, change a safety limit, an LCO [limiting condition for 
    operation], or a surveillance requirement on equipment required to 
    operate the plant. The NRC will directly approve any proposed change or 
    exemption to [Section] III.D.1.(a) of Appendix J prior to 
    implementation.
        Therefore, this change does not involve a significant reduction in 
    the margin of safety.
        Based on the Safety Analysis, it is concluded that: (1) The 
    proposed change does not constitute a significant hazards consideration 
    as defined by 10 CFR 50.92 and (2) there is reasonable assurance that 
    the health and safety of the public will not be endangered by the 
    proposed change. Moreover, because this action does not involve a 
    significant hazards consideration, it will also not result in a 
    condition which significantly alters the impact of the station on the 
    environment as described in the NRC Final Environmental Statement.
        Although the licensee has included an evaluation of a proposed 
    exemption to 10 CFR part 50, Appendix J requirements in the above 
    determination of no significant hazards consideration, only the part 
    related to the amendment is pertinent to this notice of proposed 
    amendment. The exemption request will be considered as a separate 
    matter on its own merits. The NRC staff has reviewed the licensee's 
    analysis and, based on this review, it appears that the three standards 
    of 50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: Ledyard B. Marsh
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: October 31, 1994
        Description of amendment request: The requested amendments would 
    remove the stroke times for the steam generator power operated relief 
    valves (PORVs) from Technical Specification (TS) Tables 3.6-2a and 3.6-
    2b. The PORVs are part of the main steam vent to atmosphere system. The 
    PORV actuators have difficulty developing enough closing thrust to 
    adequately overcome all of the friction loads within the valves; 
    therefore, difficulty exists in consistently meeting the present 5-
    second closing stroke time requirement. The licensee requests the 
    proposed change on the basis that the PORVs do not receive an actual 
    containment isolation signal; therefore, it is justified to remove the 
    stroke times from TS Tables 3.6-2a and 3.6-2b.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        In 48 FR 14870, the Commission has set forth examples of amendments 
    that are considered not likely to involve significant hazards 
    considerations. Example (vi) describes a change which either may result 
    in some increase to the probability or consequences of a previously-
    analyzed accident or may reduce in some way a safety margin, but where 
    the results of the change are clearly within all acceptable criteria 
    with respect to the system or component specified in the Standard 
    Review Plan. In this case, the proposed amendment is similar to example 
    (vi) in that it removes the required isolation time of the steam 
    generator PORVs from TS Tables 3.6-2a and 3.6-2b; however, no adverse 
    impact upon accident analyses is created as a result.
    Criterion 1
        The requested amendments will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The effects of the delays in isolation times on the various transients 
    affected have been analyzed and found to be acceptable. Since these 
    valves do not receive a containment isolation signal, and no credit is 
    taken for operation of these valves in the dose analysis for a 
    containment isolation function, a maximum stroke time does not apply 
    for containment isolation.
    Criterion 2
        The requested amendments will not create the possibility of a new 
    or different kind of accident from any accident previously evaluated. 
    SV PORV closure (provided the valves are not already closed at the 
    start of the transient) is a response to a transient already in 
    progress. The possibility of a spurious SV PORV opening will not be 
    affected by the requested amendments. No equipment or component 
    reconfiguration will occur as a result of this change. Finally, no 
    changes to plant procedures are being made which would affect any 
    accident causal mechanisms.
    Criterion 3
        The requested amendments will not involve a significant reduction 
    in a margin of safety. The isolation times which are applicable to 
    these valves are specified in TS Table 3.3-5, Engineered Safety 
    Features Response Times. The effects of the isolation of these valves 
    were evaluated based on their ESF function, not a containment isolation 
    function, and determined to be acceptable.
        Based upon the preceding analyses, Duke Power Company concludes 
    that the requested amendments do not involve a significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    [[Page 8746]] amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: June 13, 1994, as supplemented August 
    15, 1994.
        Description of amendment request: The proposed changes would 
    increase the initial fuel enrichment limit from a current maximum of 
    4.0 weight % to 4.75 weight % and establish new loading patterns for 
    new and irradiated fuel in the spent fuel pool to accommodate this 
    increase. These changes would also increase the efficiency of fuel 
    storage cell use in the spent fuel pools and provide additional 
    flexibility to the reload design efforts at Duke Power Company, while 
    at the same time maintaining sufficient criticality safety margin and 
    decay heat removal capabilities.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        There is no increase in the probability or consequences of an 
    accident in the new fuel vault since the only credible accidents for 
    this area are criticality accidents and it has been shown that 
    calculated, worst case Keff for this area is 0.95 under 
    all conditions.
        There is no increase in the probability of a fuel drop accident in 
    the Spent Fuel Storage Pool since the mass of an assembly will not be 
    affected by the increase in fuel enrichment. The likelihood of other 
    accidents, previously evaluated and described in Section 9.1.2 of the 
    FSAR [Final Safety Analysis Report], is also not affected by the 
    proposed changes. In fact, it could be postulated that since the 
    increase in fuel enrichment will allow for extended fuel cycles, there 
    will be a decrease in fuel movement and the probability of an accident 
    may likewise be decreased. There is also no increase in the 
    consequences of a fuel drop accident in the Spent Fuel Pool since the 
    fission product inventory of individual fuel assemblies will not change 
    significantly as a result of increased initial enrichment. In addition, 
    no change to safety related systems is being made. Therefore, the 
    consequences of a fuel rupture accident remain unchanged. Also, it has 
    been shown that keff is 0.95, under all conditions 
    therefore, the consequences of a criticality accident remain unchanged 
    as well.
        2. The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not create the possibility of a new or 
    different kind of accident since fuel handling accidents (fuel drop and 
    misplacement) are not new or different kinds of accidents. Fuel 
    handling accidents are already discussed in the FSAR for fuel with 
    enrichments up to 4.1 weight %. As described in Section VI.9 of 
    Attachment IV, additional analyses have been performed for fuel with 
    enrichment up to 4.75 weight %. Worst case misloading accidents 
    associated with the new loading patterns were evaluated. For all 
    possible misloading accidents the negative reactivity provided by 
    soluble boron maintains keff 0.95. of safety.
        3. The proposed changes do not involve a significant reduction in 
    the margin of safety.
        The proposed change does not involve a significant reduction in the 
    margin of safety since, in all cases, a keff 0.95 is 
    being maintained. Criticality analyses have been performed which show 
    that the new fuel storage vault will remain subcritical under a variety 
    of moderation conditions, from fully flooded to optimum moderation. As 
    discussed above, the Spent Fuel Pool will remain sufficiently 
    subcritical during any fuel misplacement accident.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242.
        NRC Project Director: Herbert N. Berkow.
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: November 11, 1994, as supplemented 
    January 30, 1995.
        Description of amendment request: The amendments would revise the 
    Technical Specifications Design Features section to establish 
    restricted loading patterns and associated burnup criteria for placing 
    fuel in the Oconee Spent Fuel Pools. These changes are necessary to 
    address two new fuel designs which have increased initial fuel 
    enrichment and therefore cannot be stored in the spent fuel pools under 
    existing Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Standard 1. The proposed amendments will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        Each accident analysis addressed in the Oconee Final Safety 
    Analysis Report (FSAR) has been examined with respect to changes in 
    Cycle 15 parameters to determine the effect of the Cycle 16 reload and 
    to ensure that the acceptance criteria of the FSAR safety analyses 
    remain satisfied. The transient evaluation of Cycle 16 is considered to 
    be bounded by previously accepted analyses. Section 7 of the Reload 
    Report addresses ``Accident and Transient Analysis'' for this core 
    reload.
        There is no increase in the probability or consequences of an 
    accident due to the spent fuel storage restrictions proposed in this 
    amendment request. It has been shown that the calculated, worst case 
    keff for this area is [less than or equal to] 0.95 under all 
    conditions. There is no increase in the probability of a fuel drop 
    accident in the SFP [spent fuel pool] since the mass of the new 
    assemblies is not significantly different from the mass of the old 
    assemblies. The likelihood of other accidents, previously evaluated and 
    described in the FSAR, is also not affected by the proposed changes. In 
    fact, it could be postulated that since the increase in fuel enrichment 
    will allow for extended fuel cycle lengths, there will be a decrease in 
    fuel movement and the probability of an accident may actually be 
    reduced. There is also no increase in the consequences of a fuel rod 
    drop accident in the SFP since the fission product inventory of 
    [[Page 8747]] individual fuel assemblies will not change significantly 
    as a result of increasing the initial enrichment. In addition, no 
    change to safety related systems is being made. Therefore, the 
    consequences of a fuel rupture accident remain unchanged. In addition, 
    it has been shown that keff is [less than or equal to] 0.95 under 
    all conditions. Therefore, the consequences of a criticality accident 
    in the SFP remain unchanged as well. The above analysis ensures that 
    the proposed reload amendment request will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The analyses performed in support of this reload are in accordance 
    with the NRC approved methods delineated in Specification 6.9.2. The 
    predicted operating characteristics of Oconee 3 Cycle 16 are similar to 
    previously licensed designs. The Mark B10T and Mark B11 fuel assembly 
    designs remain mechanically compatible with all fuel handling 
    equipment. Therefore, no new or different kind of fuel handling 
    accident is created by the proposed amendment request.
        Section 15.11 of the Oconee FSAR states that the refueling boron 
    concentration is maintained such that a criticality accident during 
    refueling is not considered credible. The proposed amendment request 
    continues to assure that a criticality accident in the SFP or during 
    refueling is not credible. The double contingency principle discussed 
    in ANSI N-16.1-1975 and the April 1978 NRC letter allows credit for 
    soluble boron under other abnormal or accident conditions, since only a 
    single accident need be considered at one time. Thus, by requiring a 
    minimum boron concentration in the SFP, a criticality accident caused 
    by violating the SFP storage restrictions is not considered credible. 
    Therefore, the proposed amendment request does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed changes do not involve a significant reduction in 
    the margin of safety.
        The Oconee 3 Cycle 16 design was performed using the NRC approved 
    methods given in Specification 6.9.2. The safety limits for Oconee 3 
    Cycle 16 are unchanged from previous cycles. The limits and margins 
    summarized in the Oconee 3 Cycle 16 Reload Report are well within the 
    allowable limits and requirements, and reflect no reductions to any 
    margins of safety.
        The proposed change does not involve a significant reduction in the 
    margin of safety related to SFP criticality. In all cases, a keff 
    [less than or equal to] 0.95 is maintained. Criticality analyses have 
    been performed which show that the SFP will remain sufficiently 
    subcritical during any fuel misplacement accident. In summary the 
    proposed changes do not involve a significant reduction in the margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691.
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036.
        NRC Project Director: Herbert N. Berkow.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    
        Date of amendment request: January 6, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TSs) 3/4.8.1.1, ``AC Sources-
    Operating,'' and 3/4.8.1.2, ``AC Sources-Shutdown,'' to (1) revise the 
    minimum quantity of fuel oil required in the day tanks and the storage 
    tanks, (2) add specific actions to be taken if the storage tank levels 
    fall below minimum requirements, (3) revise and relocate to the 
    associated Bases the fuel oil sampling and testing criteria, and (4) 
    add specific actions to be taken if the fuel oil properties do not meet 
    specified limits. The proposed amendment would also revise TS 6.8.4, 
    ``Programs,'' to add a requirement for a diesel fuel oil testing 
    program. The licensee stated that the proposed changes are consistent 
    with the NRC's Improved Standard Technical Specifications (NUREG-1434).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The diesel generators are not initiators or precursors to an 
    accident previously evaluated. The diesel generators are required to 
    provide onsite power to safe shutdown loads as assumed in the accident 
    analysis. Therefore, the proposed changes to the diesel generator fuel 
    oil specifications cannot significantly affect the probability of a 
    previously evaluated accident.
        The proposed change to the minimum required diesel generator fuel 
    oil levels is based on updated calculations of fuel consumption rates. 
    Because the updated calculations assume a lower consumption rate, the 
    new minimum fuel oil levels are lower but still assure that a seven-day 
    fuel oil capacity is available. Accordingly, the proposed change has no 
    effect on the operation of the diesel generator. The proposed change to 
    allow 48-hours to restore diesel generator fuel oil to the minimum 
    required level does not affect short-term diesel generator operability 
    and is acceptable based on the remaining fuel oil capacity (>6 days), 
    initiating the process for procuring additional fuel and the low 
    probability of an event requiring a diesel generator during this 
    interval. Also, the proposed allowance of a limited time to restore 
    diesel fuel oil properties to required limits will not affect the 
    short-term operability of the diesel generator. Even with minor 
    degradation of the fuel oil properties, the diesels will start and 
    perform their intended function. Relocation of the testing requirements 
    to the bases and adding a description of the Diesel Fuel Oil Testing 
    Program to the Administrative Control section are administrative 
    changes. The diesel fuel oil will continue to be sampled and tested in 
    a manner to assure its quality. In summary, the changes will not 
    adversely affect the performance or the ability of the diesel 
    generators to perform their intended function. Therefore, the proposed 
    changes will not significantly increase the consequences of an accident 
    previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes will revise the minimum required diesel 
    generator fuel oil levels and requirements associated with diesel 
    generator fuel oil properties. [[Page 8748]] The changes do not 
    introduce any new accident precursors and do not involve any 
    alterations to plant configurations which could initiate a new or 
    different kind of accident. The proposed changes do not affect the 
    short-term operability of the diesel generator. In addition, the 
    operability of the diesel generators is assured by periodic testing and 
    preventive maintenance. Therefore, the proposed changes will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        Safety margins are established through safety analyses. These 
    analyses assume that at least one diesel generator will start and load 
    whenever offsite power is lost. The proposed change to the minimum 
    required diesel generator fuel oil levels is based on updated 
    calculations of fuel consumption rates. The updated calculations use 
    the guidance delineated in Regulatory Guide 1.137 which is based on 
    time-dependent loads of the diesel-generators during design basis 
    events. Calculations based on time dependent loads result in new 
    minimum fuel oil levels which are lower. This change has no effect on 
    the operation of the diesel generator or on a margin of safety. The 
    allowance of a limited time to restore the fuel oil levels, or to 
    analyze and restore fuel oil properties to required limits, is 
    justified since the short term operability of the diesel generators is 
    not affected. Relocation of the fuel oil testing requirements to the 
    Bases does not affect the quality of the fuel oil. The 10CFR50.59 
    process will assure that future changes to the Bases will maintain the 
    current margins of safety, and that the diesel fuel oil will continue 
    to be sampled and tested in such a manner as to assure its quality. 
    Adding a description of the Diesel Fuel Oil Testing Program to the 
    Administrative Control section of Technical Specifications are 
    administrative. Therefore, the diesel generator will continue to 
    operate as analyzed and there will not be a significant reduction in a 
    margin of safety.
        The proposed changes are further justified in that they are 
    consistent with the requirements of the Improved Standard Technical 
    Specifications (NUREG-1434).
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Ledyard B. Marsh.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    
        Date of amendment request: January 6, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TSs) 3/4.3.7.5, ``Accident Monitoring 
    Instrumentation,'' and TS 3/4.4.2, ``Safety/Relief Valves.'' TS 3/
    4.3.7.5 would be revised to delete certain instruments not classified 
    as Category 1 (Type A or non-Type A) as defined in Regulatory Guide 
    1.97 and to delete the requirement that accident monitoring 
    instrumentation be operable in Operational Condition 3. The ACTIONS of 
    TS Table 3.3.7.5-1 would be revised to allow 30 days to restore one 
    inoperable channel and 7 days to restore two inoperable channels. TS 
    3.3.7.5 would be revised to add an exception to the requirements of TS 
    3.0.4. In addition, editorial changes would be made to TS Tables 
    3.3.7.5-1 and 4.3.7.5-1 for consistency and clarity.
        The proposed amendment would also revise TS 3/4.4.2 to remove 
    requirements related to safety/relief valve acoustic monitors to be 
    consistent with the proposed changes to TS Tables 3.3.7.5-1 and 
    4.3.7.5-1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of NMP2 [Nine Mile Point Nuclear Station Unit 2] in 
    accordance with the proposed amendment, will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        PAM [Post-Accident Monitoring] instruments are used to help guide 
    operator response to postulated accidents. Thus, the status or 
    operability of PAM instrumentation does not affect the probability of 
    previously analyzed accidents. The non-Category 1 PAM instruments being 
    removed from the Technical Specifications do not meet any of the 
    Commission's screening criteria and are not of controlling importance 
    to safety or necessary to obviate the possibility of an abnormal 
    situation or event giving rise to an immediate threat to public health 
    and safety. The operability of critical parameters necessary to assure 
    proper response to previously analyzed accidents (i.e., Category 1 
    instruments) is still controlled by the Technical Specifications. Thus, 
    deleting non-Category 1 instruments will not increase the consequences 
    of any accident previously evaluated.
        PAM instruments are related to the diagnosis and preplanned actions 
    required to mitigate DBAs [Design Basis Accidents] assumed to occur in 
    Operational Conditions 1 and 2. A DBA during Operational Condition 3 is 
    extremely unlikely. The requirement to maintain the Reactor Water 
    Level, Suppression Pool Water Level and Drywell High Range Radiation 
    Monitor instrumentation operable in Operational Condition 3 will be 
    deleted. Because Suppression Pool Water Level indication will no longer 
    be required in Operational Condition 3, its ACTION requirement was 
    revised to delete the requirement to place the plant in COLD SHUTDOWN, 
    Operational Condition 4. This is consistent with ITS [Improved Standard 
    Technical Specifications] which requires that the plant be brought to 
    an operational condition in which the LCO [Limiting Condition for 
    Operation] does not apply if a required action cannot be met. 
    Therefore, deleting the requirement that PAM instruments be operable 
    during Operational Condition 3 and changing the ACTION requirement for 
    Suppression Pool Water Level Monitoring does not affect the probability 
    or consequences of an accident.
        The passive nature of the Category 1 PAM instruments (i.e., those 
    instruments that initiate no critical automatic action) and the 
    alternate means available to obtain the required information assure an 
    acceptable level of safety is maintained during operation with 
    instrument channels out of service. Since an acceptable level of safety 
    is maintained with inoperable channels, plant startup or operation with 
    inoperable channels will not alter plant response to analyzed 
    accidents. Thus, the proposed changes to the required ACTIONS and the 
    proposed exemption to Specification 3.0.4 will not increase the 
    consequences of analyzed events.
        The proposed changes to the requirements for PCIV [Primary 
    [[Page 8749]] Containment Isolation Valve] indication are consistent 
    with the proposed required ACTIONS. Position indication will still be 
    required for each operable PCIV and penetrations without adequate PCIV 
    indication status will be isolated, thus assuring containment integrity 
    in the event of an accident. Deletion of the ``Minimum Required 
    Actions'' column in Table 3.3.7.5-1 is consistent with the proposed 
    ACTIONS for LCO 3.3.7.5, since compensatory actions are based on 
    compliance with the ``Required Number of Channels.'' Deleting the 
    ``Applicable Operating Conditions'' column is consistent with the 
    proposed changes and other NMP2 Technical Specifications sections. 
    Finally, referencing Specification 4.0.5 is an administrative change 
    which does not alter any existing surveillance requirements for the 
    safety relief valves.
        In aggregate, the proposed changes do not affect the plant in a way 
    that could directly contribute to causing or mitigating the effects of 
    an accident. Therefore, the operation of NMP2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The operation of NMP2, in accordance with the proposed amendment, 
    will not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes do not represent a physical change to the 
    plant as described in the NMP2 USAR [Updated Safety Analysis Report]. 
    The proposed changes do not modify any plant equipment and the initial 
    conditions used for the design basis accident analysis are still valid. 
    Thus, no potential initiating events are created which would cause any 
    new or different kinds of accidents. PAM instrumentation is used to 
    guide operator response during postulated accidents. Those PAM 
    instruments considered of controlling importance to safety are retained 
    in the Technical Specifications. Thus, plant response to previously 
    analyzed events is not altered so as to create any new or different 
    kinds of accidents. Therefore, operation of Nine Mile Point Unit 2 in 
    accordance with the proposed change will not create the possibility of 
    a new or different kind of accident from any previously assessed.
        The operation of NMP2, in accordance with the proposed amendment, 
    will not involve a significant reduction in a margin of safety.
        The non-Category 1 PAM instruments being removed from the Technical 
    Specifications do not meet any of the Commission's screening criteria. 
    That is, the instruments being proposed for removal are not of 
    controlling importance to safety or necessary to obviate the 
    possibility of an abnormal situation or event giving rise to an 
    immediate threat to public health and safety. Thus, they are not 
    critical to any margin of safety.
        PAM instruments are related to the diagnosis and preplanned actions 
    required to mitigate DBAs assumed to occur in Operational Conditions 1 
    and 2. A DBA during Operational Condition 3 is extremely unlikely. The 
    requirement to maintain the Reactor Water Level, Suppression Pool Water 
    Level and Drywell High Range Radiation Monitor instrumentation operable 
    in Operational Condition 3 will be deleted. Because Suppression Pool 
    Water Level indication will no longer be required in Operational 
    Condition 3, its ACTION requirement was revised to delete the 
    requirement to place the plant in COLD SHUTDOWN, Operational Condition 
    4. This is consistent with the ITS, which requires that the plant be 
    brought to an operational condition in which the LCO does not apply if 
    a required action cannot be met. Therefore, deleting the requirement 
    that PAM instruments be operable during Operational Condition 3 and 
    changing the ACTION requirement for Suppression Pool Water Level 
    Monitoring does not significantly reduce a margin of safety.
        Since the Category 1 PAM instruments are passive in nature (i.e., 
    no critical automatic action is assumed to occur from these 
    instruments) and alternate means exist to obtain the required 
    information, an acceptable level of safety is assured when instrument 
    channels are out of service. Also, the probability of an event 
    requiring PAM instrumentation is low. Continued operation with one 
    channel out of service, and limited plant operation with two channels 
    out of service, does not compromise plant safety margins. An acceptable 
    level of safety is maintained during plant startups and operation with 
    instrument channels out of service. Thus, the proposed changes to the 
    required ACTIONS and the proposed exemption to Specification 3.0.4 will 
    not significantly reduce a margin of safety.
        The proposed changes to PCIV indication will assure correct 
    implementation of the ACTIONS discussed above. Isolating the flow path 
    associated with one or two inoperable PCIV indication channels is 
    conservative since the subject valve will be positioned as required to 
    assure primary containment integrity. The remaining editorial changes 
    are administrative in nature and by definition do not affect safety 
    margins. Deleting the ``Minimum Operable Channels'' and ``Applicable 
    Operating Conditions'' columns is consistent with the proposed changes. 
    Finally, referencing the requirements of Specification 4.0.5 is an 
    administrative change and by definition does not reduce the margin of 
    safety.
        Therefore, the operation of NMP2 in accordance with the proposed 
    change will not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Ledyard B. Marsh.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: December 9, 1994.
        Description of amendment request: The proposed changes incorporate 
    NRC recommendations contained in Generic Letter 93-05 related to the 
    diesel generator (DG) surveillance requirements and other DG 
    surveillance requirements related to the cold starts. The proposed 
    changes to the DG operability testing surveillance requirements are 
    consistent with the intent of GL 93-05 however vary in some 
    particulars, because of circumstances specific to Millstone 3. The 
    proposed changes will modify the requirement for the DG operability 
    testing when the other DG is inoperable, delete the requirement for DG 
    operability testing when one or both offsite AC sources are inoperable, 
    eliminate fast loading of DGs except for the 18-month test, and modify 
    the hot restart test from the 24-hour loaded test run for the DGs.
        Basis for proposed no significant hazards consideration 
    determination: [[Page 8750]] As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration (SHC), which is presented below:
    
    * * * The proposed changes do not involve a SHC because the changes 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed changes revise the action requirements regarding 
    operability testing of a non-affected DG when the other DG is 
    inoperable, delete the requirement for operability testing of the DGs 
    when one or both offsite AC sources are inoperable and eliminate the 
    fast loading of DGs except for the 18-month test. These changes will 
    improve DGs performance by reducing the number of unnecessary quick 
    starts and by requiring more appropriate testing of the DGs when there 
    is a potential for common mode failure. The proposed change, to revise 
    the method of verifying DG hot restart capability after a 24-hour run 
    without loading the DG with LOP/SI [loss of offsite power/safety 
    injection] load, meets an intent of Regulatory Guide 1.108, Position 
    C.2.a.5, which states the purpose of the test as to ``demonstrate 
    functional capability at full load temperature conditions.'' Functional 
    capability of the DG can be adequately demonstrated by manually or 
    automatically restarting the DG within five minutes after a 24-hour 
    test run without loading it with LOP/SI loads, provided that a full 
    load temperature condition is maintained prior to restart. The proposed 
    DG restart method does not reduce the effectiveness of the test. The 
    proposed revisions of the DG surveillance requirements will not 
    increase the probability of an accident and it will not change the 
    response of the DG to a LOP as described in the Millstone Unit No. 3 
    FSAR. Since the plant response to an accident will not change, there is 
    no change in the potential for an increase in the consequences of an 
    accident previously analyzed.
        2. Create the possibility of a new or different kind of an accident 
    previously evaluated.
        The proposed changes of the DG surveillance requirements and 
    operability testing requirements do not affect the operation or 
    response of any plant equipment or introduce any new failure 
    mechanisms. The proposed changes do not affect the test results and the 
    DGs will be verified to be operable and their response to a loss of 
    voltage will be unchanged. The plant equipment will respond per the 
    design and analyses and there will not be a malfunction of a new or any 
    type introduced by the revision to the DG surveillance requirements. As 
    such, the changes do not create the possibility of a new or different 
    kind of accident previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The bases of Technical Specification 3/4.8, ``Electrical Power 
    Systems,'' state that the operability of the AC and DC power systems 
    and associated distribution systems ensure that sufficient power will 
    be available to supply the safety-related equipment required for safe 
    shut down and mitigation and control of accident conditions. The bases 
    also state that the surveillance requirements for determining the 
    operability of the DGs are in accordance with the recommendations of 
    Regulatory Guide 1.108, Revision 1. The revisions of the surveillance 
    requirements establishes tests that will continue to verify that the 
    DGs are operable and the testing will still meet the intent of 
    Regulatory Guide 1.108, Revision 1. Operable DGs ensure that the 
    assumptions in the bases of the Technical Specifications are not 
    affected and ensure that the margin of safety is not reduced. 
    Therefore, the assumptions in the bases of the technical specifications 
    are not affected and these changes do not result in a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: December 14, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Millstone Unit No. 3 Technical Specifications by:
        1. Increasing the upper bound of the overall containment integrated 
    leakage rate required by Technical Specification 3.6.1.2.a from 0.3 wt. 
    % per day to 0.65 wt. % per day of the containment air per 24 hours at 
    design basis pressure.
        2. Revising Technical Specification 4.6.6.1.d.3 by providing more 
    margin with respect to the drawdown time for secondary containment 
    vacuum.
        3. Revising Bases Section 3/4.7.9 to reflect the above changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
    * * * The proposed changes do not involve an SHC because the changes 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
    
    * * * There is a reasonable assurance that the modified criteria for 
    the negative pressure in the secondary containment boundary proposed 
    via the proposed change (i.e., a negative pressure of 0.1 inches in one 
    minute and a negative pressure of 0.4 inches within the next two 
    minutes), can be accomplished in the prescribed time.
        Extension of the time allowed to achieve the final drawdown of 
    secondary containment from 120 seconds to 180 seconds (these times 
    include the diesel generator start and load time of approximately 11 
    seconds) will have a negligible impact on heating and cooling. Plant 
    experience has shown that heatup and cooldown of thick-walled concrete 
    structures, such as the Millstone Unit No. 3 auxiliary building, is a 
    relatively slow process. Also, natural convection within the auxiliary 
    building tends to stabilize temperatures. Following an accident signal, 
    ventilation equipment is restarted promptly. Therefore, heatup or 
    cooldown, during short periods while ventilation fans and/or heaters 
    are inactive, is insignificant and can be neglected.
        The proposed change to reinstate the containment integrated leakage 
    rate at the design basis pressure from 0.3 wt % per day to 0.65 wt % 
    per day has been evaluated to determine the impact to the Appendix J 
    requirements for Type A, B and C Testing. In addition, the radiological 
    consequence evaluation also addressed the increase in La (i.e., 
    from 0.3 wt % per day to 0.65 wt % per day).
        On October 12, 1993, Millstone Unit No. 3 successfully conducted 
    the second [[Page 8751]] Type A test in the first 10-year service 
    period. Test results indicated that the ``As-Found'' and ``As-Left'' 
    ILRTs [integrated leakage rate tests] passed the technical 
    specification acceptance criteria. The ``As-Found'' value was 0.1327 
    weight percent per day and the ``As-Left'' value was 0.1313 weight 
    percent per day. These values represent 27.2% and 26.9% of the 
    technical specification criterion of 0.4875 wt % per day (0.75 
    La), based on La equal to 0.65 wt % per day, respectively. In 
    addition, as of October 9, 1993, the total Type B and C ``As-Found'' 
    and ``As-Left'' leakage results were 0.099 wt % per day, and 0.084 wt % 
    per day, respectively. These values represent approximately 25.3% and 
    21.5% of the technical specification limit of 0.39% wt % per day (0.6 
    La), based on La equal of 0.65 wt % per day, respectively. 
    Correspondingly, the 1993 Type A, B, and C test results indicate that 
    the ``As-Found'' and ``As-Left'' result in each test case was below the 
    existing Technical Specification limit of 0.3 wt % per day. This 
    further demonstrates the overall leakage integrity of the containment 
    and its boundaries.
        Based on the relatively low ``As-Left'' ILRT leakage rate (i.e., 
    0.1313 wt % per day is well below the existing technical specification 
    limit of 0.225 wt % per day (0.75 La), based on La equal to 
    0.3 wt % per day), which represents the overall containment integrated 
    leakage rate for the containment prior to start-up, there is reasonable 
    assurance that containment integrity will be maintained below the 
    allowable leakage rate limit of 0.65 wt % per day. In addition, the 
    total Type B and C ``As-Left'' leakage result of 0.084 wt % per day 
    (this is well below the existing technical specification limit of 0.18 
    wt % per day (0.6 La), based on La equal to 0.3 wt % per 
    day), provides further assurance that leakage, based on individual 
    penetration, will be maintained within sufficient margin of the leakage 
    limits.
        Because the last Type A, B, and C tests were performed under the 
    technical specification limit of 0.65 wt % per day, the proposed change 
    to restore La to 0.65 wt % per day has no impact to these systems 
    from a leakage allowance perspective. As indicated above, the previous 
    test results met the technical specification leakage limits (based on 
    0.65 wt % per day) within sufficient margin and, therefore, would not 
    present any challenge to these leakage limits.
        NNECO has evaluated the proposed changes to Surveillance 
    Requirement 4.6.6.1.d.3 that increase the time to draw a final required 
    negative pressure as measured at the 24'-6'' elevation of the auxiliary 
    building in conjunction with the proposed change to reinstate the 
    containment integrated leakage rate of 0.65 wt % per day to determine 
    the impact on the offsite doses following a LOCA. The calculated 
    radiological doses are, in most cases, less than the previously 
    calculated doses (i.e., EAB [exclusion area boundary] and LPZ [low-
    population zone] doses) and are within the 10CFR100 limits. Previously, 
    the EAB thyroid and whole body doses as documented in the November 4, 
    1993, submittal were calculated to be 141 REM and 9.4 REM respectively, 
    while the previously docketed (i.e., the November 4, 1993, submittal) 
    LPZ doses to the thyroid and whole body were calculated to be 29.8 REM 
    and 1.7 REM respectively. Utilizing the revised application of 
    containment recirculation spray DF, the EAB thyroid and whole body 
    doses were calculated to be 61 REM and 16.7 REM, respectively, and the 
    LPZ thyroid and whole body doses were calculated to be 10.9 REM and 2.8 
    REM respectively. The assumptions used in the above radiological dose 
    calculations are provided in Attachment 1. It is noted that a LOCA at 
    Millstone Unit No. 3 is also one of the bounding accidents for the 
    Millstone Unit No. 3 control room, Millstone Unit No. 2 control room, 
    and the Millstone Technical Support Center habitability analysis. 
    Therefore, the doses for these areas were recalculated and are 
    presented in the Safety Assessment section above. The Millstone Unit 
    No. 1 control room and the Emergency Operating Facility doses are 
    bounded by the Millstone Unit No. 1 LOCA calculations.
        The Millstone Unit Nos. 2 and 3 control rooms and Millstone 
    Technical Support Center doses were not recalculated in 1993 (i.e., 
    November 4, 1993, submittal) since EAB/LPZ doses proved that the 
    releases were less than the 1990 submittal. In summary, all control 
    room and Technical Support Center doses are within the guidelines of 
    GDC 19. Therefore, the proposed changes do not result in an increase in 
    consequences of an accident (i.e., a LOCA) previously analyzed.
        The proposed changes to Bases Section 3/4.6.6 do not have any 
    safety impact since they only reflect the changes proposed to 
    Surveillance Requirement 4.6.6.1.d.3.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes do not compromise the ability of the SLCRS 
    [supplementary leak collection and release system] and ABFS [auxiliary 
    building filter system] to mitigate the consequences of an accident. 
    The proposed changes do not make any physical or operational changes to 
    existing plant structures, systems or components. The proposed changes 
    do not introduce any new or unique operational modes or accident 
    precursors. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        NNECO has evaluated the proposed changes to Surveillance 
    Requirement 4.6.6.1.d.3 that increase the time to draw a final required 
    negative pressure as measured at the 24'-6'' elevation of the auxiliary 
    building in conjunction with the proposed change to reinstate the 
    containment integrated leakage rate of 0.65 wt % per day to determine 
    the impact on the offsite doses following a LOCA. The calculated 
    radiological doses are, in most cases, less than the previously 
    calculated doses and these doses are within the 10CFR100 limits. All 
    control rooms and technical support center doses are within the 
    guidelines of GDC 19. Therefore, the proposed changes do not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: December 23, 1994.
        Description of amendment request: The proposed amendment would 
    change the acceptance criteria for the peak transient generator voltage 
    from 4784 volts to 5000 volts during full load rejection tests of the 
    diesel generator (DG), and delete the 10-year surveillance requirement 
    to perform a [[Page 8752]] 110% pressure test of the DG fuel oil 
    system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
    * * * The proposed changes do not involve a SHC because the changes 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
    DG Full-Load Rejection Test
        NNECO is proposing to modify Surveillance Requirement 4.8.1.1.2.g.3 
    of the Millstone Unit No. 3 Technical Specifications by changing the 
    acceptable transient voltage to 5000 volts from 4784 volts. This change 
    will permit the DG full load rejection tests to be performed at 
    realistic plant conditions using a power factor that will envelope the 
    calculated power factor during the worst kW loading conditions. The 
    transient voltage of 5000 volts is within the normal design limits of 
    the DGs.
        The proposed change does not alter the intent of the surveillance, 
    does not involve any physical changes to the plant, does not alter the 
    way any structure, system, or component functions, and does not modify 
    the manner in which the plant is operated. As such, the proposed change 
    to Surveillance Requirement 4.8.1.1.2.g.3 will not degrade the 
    capability of the DGs to perform their intended safety function, and 
    will not reduce the availability of the DGs. Actually, the proposed 
    change will increase the effectiveness of the full load rejection 
    tests, because the DGs will be tested in a configuration that is closer 
    to the design basis conditions.
    Pressure Test of the DG Fuel Oil System
        The DG fuel oil system is classified as an ASME Code Class 3 system 
    in accordance with the guidance of Regulatory Guide 1.26, ``Quality 
    Group Classification and Standards for
    Water-, Steam-, and Radioactive-waste Components of Nuclear Power 
    Plants.'' Surveillance Requirement 4.0.5 requires the testing of ASME 
    Class 1, 2, and 3 components in accordance with Section XI of the ASME 
    Code. Surveillance Requirement 4.8.1.1.2.i.2 is redundant to the ASME 
    Section XI pressure test requirements of Surveillance Requirement 
    4.0.5. Additionally, the DG fuel oil tank cannot be tested in the 
    configuration required by Surveillance Requirement 4.8.1.1.2.i.2, 
    because the tanks are vented to the atmosphere and the vent cannot be 
    isolated. Therefore, NNECO is proposing to delete Surveillance 
    Requirement 4.8.1.1.2.i.2.
        The proposed change does not modify the manner in which the DGs 
    respond to an accident. Also, the proposed change does not reduce the 
    reliability of the DGs.
    Conclusion
        Based on the above, the proposed changes to Surveillance 
    Requirements 4.8.1.1.2.g.3 and 4.8.1.1.2.i.2 of the Millstone Unit No. 
    3 Technical Specifications do not involve a significant increase in the 
    probability or consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
    DG Full-Load Rejection Test
        The DGs are required to operate in response to a loss of offsite 
    power. Their failure cannot initiate an accident. Additionally, the 
    proposed change to Surveillance Requirement 4.8.1.1.2.g.3 does not 
    affect the operation or response of any plant structure, system, or 
    component, and it does not introduce any new failure mechanisms.
    Pressure Test of the DG Fuel Oil System
        The proposed change to Surveillance Requirement 4.8.1.1.2.i.2 does 
    not affect the design or function of the DG fuel oil system. Failure of 
    the DG fuel oil system would not initiate an accident.
    Conclusion
        Based on the above, the proposed changes to Surveillance 
    Requirements 4.8.1.1.2.g.3 and 4.8.1.1.2.i.2 of the Millstone Unit No. 
    3 Technical Specifications will not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Involve a significant reduction in the margin of safety.
    DG Full-Load Rejection Test
        NNECO is proposing to modify Surveillance Requirement 4.8.1.1.2.g.3 
    of the Millstone Unit No. 3 Technical Specifications by changing the 
    acceptable transient voltage to 5000 volts from 4784 volts. The intent 
    of the proposal is to permit the DG full load rejection tests to be 
    conducted at conditions which simulate design basis conditions.
        The proposed change does not alter the intent of the surveillance, 
    does not involve any physical changes to the plant, does not alter the 
    way any structure, system, or component functions, and does not modify 
    the manner in which the plant is operated. As such, the proposed change 
    to Surveillance Requirement 4.8.1.1.2.g.3 will not degrade the ability 
    of the DGs to perform their intended safety function, and will not 
    reduce the availability of the DGs.
        The bases of Technical Specification 3/4.8, ``Electrical Power 
    Systems,'' state that the operability of the AC and DC power systems 
    and associated distribution systems ensure that sufficient power will 
    be available to supply the safety related equipment required for safe 
    shutdown and for the mitigation of transients. The proposed change to 
    the surveillance requirement will increase the effectiveness of the 
    full load rejection tests.
        This will ensure the operability of the DGs. Operable DGs ensure 
    that the assumptions for the bases of the Millstone Unit No. 3 
    Technical Specifications are not affected.
    Pressure Test of the DG Fuel Oil System
        NNECO is proposing to delete Surveillance Requirement 4.8.1.1.2.i.2 
    from the Millstone Unit No. 3 Technical Specifications. This 
    surveillance requirement is redundant to the requirements of 
    Surveillance Requirement 4.0.5 which invokes ASME Section XI. 
    Additionally, the fuel oil system cannot be tested to the requirements 
    of Surveillance Requirement 4.8.1.1.2.i.2 because the DG fuel oil tanks 
    are vented to the atmosphere and this vent path cannot be isolated.
        Millstone Unit No. 3 will include the DG fuel oil system pressure 
    test as an augmented inspection within the Inservice Inspection 
    program. Inspections will be performed in compliance with the 
    requirement of the 1983 Edition of ASME Section XI, Table IWD-2500-1, 
    ``Test and Examination Categories.'' Testing (i.e., a system 
    hydrostatic test) in accordance with ASME Section XI will provide 
    equivalent assurance of tank and piping integrity.
    Conclusion
        Based on the above, the proposed changes to Surveillance 
    Requirements 4.8.1.1.2.g.3 and 4.8.1.1.2.i.2 of the Millstone Unit No. 
    3 Technical Specifications do not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    [[Page 8753]] amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: January 18, 1995.
        Description of amendment request: The proposed changes to the 
    technical specifications will increase the minimum required boron 
    concentration in the boric acid tank (BAT) from 6300 ppm to 6600 ppm.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
    * * * The proposed changes do not involve an SHC because the changes 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The change affects the minimum required boron concentration in the 
    BAT. Changes in the tank's boron concentration will not affect the 
    probability of any plant accident.
        An increase in the minimum BAT concentration of 6600 ppm was 
    recommended by Westinghouse based on their Cycle 6 BORDER evaluation. 
    The BORDER evaluation conservatively determines the ability to maintain 
    shutdown margin when the plant is taken from an initial operating 
    condition of Mode 1 or 2 to a final condition of Mode 5 or 6 using an 
    assumed minimum BAT concentration. Therefore, the ability to maintain 
    shutdown margin is assured and the change will not adversely affect the 
    consequences of any plant accident.
        2. Create the possibility of a new or different kind of accident 
    from any Previously Analyzed.
        The change conservatively increases the minimum required boron 
    concentration in the BAT from 6300 ppm to 6600 ppm. There is no impact 
    on the operability of plant systems or equipment. Therefore, the change 
    does not create a malfunction that is different from those previously 
    evaluated.
        3. Involve a significant reduction in the margin of safety.
        The proposed increase in the minimum boron concentration in the BAT 
    provides conservatism in the calculated shutdown margin for Millstone 
    Unit No. 3. The change does not adversely affect any equipment credited 
    in the safety analysis. Also, the change does not adversely affect the 
    probability or consequences of any plant accident, including the 
    calculated PCT [peak clad temperature] or offsite doses. Therefore, 
    there is no impact on the margin of safety as specified in the 
    Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County, 
    Minnesota
    
        Date of amendment requests: January 10, 1995.
        Description of amendment requests: The proposed amendments would 
    revise the Prairie Island Event Monitoring Instrumentation Technical 
    Specifications and associated Bases to conform to Standard Technical 
    Specifications for post-accident monitoring.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        The primary purpose of post accident monitoring instrumentation is 
    to display plant variables that provide information to the control room 
    operators during accident situations. Plant instrumentation was 
    evaluated for importance for this function when Regulatory Guide 1.97 
    [''Instrumentation for Light Water Cooled Nuclear Power Plants to 
    Assess Plant Conditions During and Following an Accident''] 
    classifications were determined. The Prairie Island Regulatory Guide 
    1.97 classification of instruments was previously approved by the NRC 
    on October 18, 1985. This amendment request proposes to base Prairie 
    Island Technical Specifications on the results of the Regulatory Guide 
    1.97 evaluation in accordance with the guidance of the industry 
    standard.
        Revising the allowed outage time for these instruments will not 
    significantly increase the probability or consequences of an accident 
    since these instruments do not initiate automatic actions, there are 
    available backup indications and the probability of an event requiring 
    these instruments to be operable is very low.
        Therefore, the probability or consequences of an accident 
    previously evaluated are not affected by any of the proposed 
    amendments.
        2. The proposed amendment[s] will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The license amendment request proposes to add instruments to the 
    Technical Specifications which have been previously determined to be 
    important for post accident monitoring, and to remove instruments from 
    Technical Specifications which have been previously determined to be 
    less important for post accident monitoring. This amendment ensures the 
    control room operators are provided with the instrumentation required 
    to properly manage an accident situation.
        Therefore, based on the above considerations, the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated would not be created.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety.
        The post accident monitoring functions do not initiate any 
    automatic actions. The instrumentation to be added to the Event 
    Monitoring Instrumentation Table was previously recognized through the 
    Regulatory Guide 1.97 evaluation process as important for post accident 
    monitoring and would be relied upon if there were an event without this 
    license amendment. Instrumentation to be removed from Technical 
    Specifications was previously recognized to be less 
    [[Page 8754]] important and would not be relied upon very much in an 
    event. Overall, with the trade-off of adding and deleting 
    instrumentation, the margin of safety will not be significantly 
    affected.
        The proposed license amendment will increase the allowed outage 
    time for most of the instruments. Again, these instruments do not 
    provide automatic actions, they provide indications for monitoring post 
    accident conditions. All of the instruments have backup or 
    corroborating indications which could be relied upon if the Technical 
    Specifications instruments were inoperable. Also, an event requiring 
    use of these instruments has a very low probability. For these reasons 
    the proposed changes in allowed outage time will not result in a 
    significant reduction in the margin of safety.
        For these same reasons, the proposed changes in radiation 
    instrument surveillance requirements will not significantly reduce the 
    margin of safety.
        Overall, a significant reduction in the margin of safety would not 
    result from this license amendment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: January 25, 1995.
        Description of amendment request: The proposed Technical 
    Specification change would replace a specific requirement for the 
    frequency of Type A tests with a general requirement to perform Type A 
    tests. The proposed amendment would change Surveillance Requirement 
    4.6.1.2.a. Specifically, the change would require the performance of 
    Type A tests (overall containment integrated leak rate tests (ILRTs)) 
    at intervals as specified in 10 CFR 50, Appendix J, instead of on a 
    specific schedule for performance of ILRTs of ``40 plus or minus 10 
    months.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 CFR 
    50.92(c)(1)) because the proposed change merely replaces a prescriptive 
    schedule for performing ILRTs with a requirement to conduct the ILRTs 
    on a schedule consistent with the Commission's regulations. The change 
    does not alter the methodology, frequency, or acceptance criteria for 
    ILRTs, does not affect the design basis of the containment, and does 
    not change the post-accident response of the containment.
        B. The change does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because the change does not affect the manner by which the 
    facility is operated and does not make any changes to existing plant 
    structures, systems, or components. The proposed change merely replaces 
    a prescriptive schedule for performing ILRTs with a requirement to 
    conduct the ILRTs on a schedule consistent with the Commission's 
    regulations.
        C. The change does not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)) because the proposed change does not 
    affect the manner by which the facility is operated or involve changes 
    to equipment or features which affect the operational characteristics 
    of the facility.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Exeter Public Library, 47 
    Front Street, Exeter, NH 03833.
        Attorney for licensee: Thomas Dignan, Esquire, Ropes & Gray, One 
    International Place, Boston, MA 02110-2624.
        NRC Project Director: Phillip F. McKee.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
    364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, 
    Alabama
    
        Date of amendments request: December 7, 1994.
        Description of amendments request: The amendments would provide a 
    permanent voltage-based steam generator tube repair criteria for both 
    units. This criteria is based on the guidance contained in the NRC 
    Proposed Generic Communication (Generic Letter 94-XX), ``Voltage-Based 
    Repair Criteria for the Repair of Westinghouse Steam Generator Tubes 
    Affected by Outside Diameter Stress Corrosion Cracking,'' that was 
    issued for public comment in the Federal Register (59 FR 41520) on 
    August 12, 1994. The licensee's submittal also includes responses to 
    and identifies exceptions taken to the draft Generic Letter. The 
    significant exceptions are: (1) The requirement to reinspect all tubes 
    if bobbin probe wear exceeds 15%; (2) the 1 x 10-2 limit on the 
    calculated conditional burst probability; and (3) the need to pull 
    additional steam generator tubes to evaluate the current condition of 
    the steam generator tubes. In addition, the operational leakage 
    requirement for Unit 2 will be modified to reduce the total allowable 
    primary-to-secondary leakage for any steam generator from 500 gallons 
    per day (gpd) to 150 gallons per day.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of Farley units in accordance with the proposed 
    license amendment does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Testing of model boiler specimens for free standing tubes at room 
    temperature conditions shows burst pressures as high as approximately 
    5000 psi for indications of outer diameter stress corrosion cracking 
    with voltage measurements as high as 26.5 volts. Burst testing 
    performed on pulled tubes with up to 7.5 volt indications show burst 
    pressures in excess of 5900 psi at room temperature. As stated earlier, 
    tube burst criteria are inherently satisfied during normal operating 
    conditions by the presence of the tube support plate. Furthermore, 
    correcting for the effects of temperature on material properties and 
    minimum strength levels (as the burst testing was [[Page 8755]] done at 
    room temperature), tube burst capability significantly exceeds the R.G. 
    [Regulatory Guide] 1.121 criterion requiring the maintenance of a 
    margin of 1.43 times the steam line break pressure differential on tube 
    burst if through-wall cracks are present without regard to the presence 
    of the tube support plate. Considering the existing data base, this 
    criterion is satisfied with bobbin coil indications with signal 
    amplitudes over twice the 2.0 volt voltage-based repair criteria, 
    regardless of the indicated depth measurement. This structural limit is 
    based on a lower 95% confidence level limit of the data. The 2.0 volt 
    criterion provides an extremely conservative margin of safety to the 
    structural limit considering expected growth rates of outside diameter 
    stress corrosion cracking at Farley. Alternate crack morphologies can 
    correspond to a voltage so that a unique crack length is not defined by 
    a burst pressure to voltage correlation. However, relative to expected 
    leakage during normal operating conditions, no field leakage has been 
    reported from tubes with indications with a voltage level of under 7.7 
    volts for 3/4 inch tube which correlates to 10 volts for 7/8 inch 
    tubing (as compared to the 2.0 volt proposed voltage-based tube repair 
    limit). Thus, the proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident.
        Relative to the expected leakage during accidents (sic) condition 
    loadings, the accidents that are affected by primary-to-secondary 
    leakage and steam release to the environment are Loss of External 
    Electrical Load and/or Turbine Trip, Loss of All AC Power to Station 
    Auxiliaries, Major Secondary System Pipe Failure, Steam Generator Tube 
    Rupture, Reactor Coolant Pump Locked Rotor, and Rupture of a Control 
    Rod Drive Mechanism Housing. Of these, the Major Secondary System Pipe 
    Failure is the most limiting for Farley in considering the potential 
    for off-site doses. The offsite doses analyses for the other events 
    which model primary-to-secondary leakage and steam releases from the 
    secondary side to the environment assume that the secondary side 
    remains intact. The steam generator tubes are not subjected to a 
    sustained increase in differential pressure, as is the case following a 
    steam line break event. This increase in differential pressure is 
    responsible for the postulated increase in leakage and associated 
    offsite doses following a steam line break event. In addition, the 
    steam line break event results in a bypass of containment for steam 
    generator leakage. Upon implementation of the voltage-based repair 
    criteria, it must be verified that the expected distributions of 
    cracking indications at the tube support plate intersections are such 
    that primary-to-secondary leakage would result in site boundary dose 
    within the current licensing basis. Data indicate that a threshold 
    voltage of 2.8 volts could result in through-wall cracks long enough to 
    leak at steam line break conditions. Applications of the proposed 
    repair criteria requires that the current distribution of a number of 
    indications versus voltage be obtained during the refueling outages. 
    The current voltage is then combined with the rate of change in voltage 
    measurement and a voltage measurement uncertainty to establish an end 
    of cycle voltage distribution and, thus, leak rate during steam line 
    break pressure differential. The leak rate during a steam line break is 
    further increased by a factor related to the probability of detection 
    of the flaws. If it is found that the potential steam line break 
    leakage for degraded intersections planned to be left in service 
    coupled with the reduced specific activity levels allowed result in 
    radiological consequences outside the current licensing basis, then 
    additional tubes will be plugged or repaired to reduce steam line break 
    leakage potential to within the acceptance limit. Thus, the 
    consequences of the most limiting design basis accident are constrained 
    to present licensing basis limits.
        (2) The proposed license amendment does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        Implementation of the proposed voltage-based tube support plate 
    elevation steam generator tube repair criteria does not introduce any 
    significant changes to the plant design basis. Use of the criteria does 
    not provide a mechanism that could result in an accident outside of the 
    region of the tube support plate elevations. Neither a single or 
    multiple tube rupture event would be expected in steam generator in 
    which the repair criteria have been applied during all plant 
    conditions. The bobbin probe signal amplitude repair criteria are 
    established such that operational leakage or excessive leakage during a 
    postulate steam line break condition is not anticipated. Southern 
    Nuclear has previously implemented a maximum leakage limit of 140/150 
    gpd (Unit 1/Unit 2) per steam generator. The R.G. 1.121 criterion for 
    establishing operational leakage limits that require plant shutdown are 
    based upon leak-before-break considerations to detect a free span crack 
    before potential tube rupture. The 140/150 gpd limit provides for 
    leakage detection and plant shutdown in the event of the occurrence of 
    an unexpected single crack resulting in leakage that is associated with 
    the longest permissible crack length. R.G. 1.121 acceptance criteria 
    for establishing operating leakage limits are based on leak-before-
    break considerations such that plant shutdown is initiated if the 
    leakage associated with the longest permissible crack is exceeded. The 
    longest permissible crack is the length that provides a factor safety 
    of 1.43 against bursting at steam line break pressure differential. A 
    voltage amplitude of approximately 9 volts for typical outside diameter 
    stress corrosion cracking corresponds to meeting this tube burst 
    requirement at the 95% prediction interval on the burst correlation. 
    Alternate crack morphologies can correspond to a voltage so that a 
    unique crack length is not defined by the burst pressure versus voltage 
    correlation. Consequently, typical burst pressure versus throughwall 
    crack length correlations is used below to define the ``longest 
    permissible crack'' for evaluating operating leakage limits.
        The single through-wall crack lengths that results in tube burst at 
    1.43 times steam line break pressure differential and steam line break 
    conditions are about 0.53 inch and 0.84 inch, respectively. Normal 
    leakage for these crack lengths would range from about 0.4 gallons per 
    minute to 4.5 gallons per minute, respectively, while lower 95% 
    confidence level leak rates would range from about 0.06 gallons per 
    minute to 0.6 gallons per minute, respectively.
        An operating leak rate of 140/150 gpd per steam generator has been 
    implemented. This leakage limit provides for detection of 0.4 inch long 
    cracks at nominal leak rates and 0.6 inch long cracks at the lower 95% 
    confidence level leak rates. Thus, the 140/150 gpd limit provides for 
    plant shutdown prior to reaching critical crack lengths for steam line 
    break conditions at leak rates less than 95% confidence level and for 
    three times normal operating pressure differential at less than nominal 
    leak rates.
        Considering the above, the implementation of voltage-based plugging 
    criteria will not create possibility of a new or different kind of 
    accident from any previously evaluated.
        (3) The proposed license amendment does not involve a significant 
    reduction in margin of safety.
        The use of the voltage-based tube support plate elevation repair 
    criteria is demonstrated to maintain steam [[Page 8756]] generator tube 
    integrity commensurate with the requirements of R.G. 1.121. R.G. 1.121 
    describes a method acceptable to the NRC staff for meeting GDCs 
    [General Design Criteria] 2, 14, 15, 31, and 32 by reducing the 
    probability of the consequences of steam generator tube rupture. This 
    is accomplished by determining the limiting conditions of degradation 
    of steam generator tubing, as established by inservice inspection, for 
    which tubes with unacceptable cracking should be removed from service. 
    Upon implementation of the criteria, even under the worst case 
    conditions, the occurrence of outside diameter stress corrosion 
    cracking at the tube support plant elevations is not expected to lead 
    to a steam generator tube rupture event during normal or faulted plant 
    conditions. The most limiting effect would be a possible increase in 
    leakage during a steam line break event. Excessive leakage during a 
    steam line break event, however, is precluded by verifying that, once 
    the criteria are applied, the expected end of cycle distribution of 
    crack indications at the tube support plate elevations would result in 
    minimal, and acceptable primary to secondary leakage during the event 
    and, hence, help to demonstrate radiological conditions are less than 
    an appropriate fraction of the 10 CFR 100 guideline.
        The margin to burst for the tubes using the voltage-based repair 
    criteria is comparable to that currently provided by existing technical 
    specifications.
        In addressing the combined effects of LOCA [loss-of-coolant 
    accident] + SSE [safe shutdown earthquake] on the steam generator 
    component (as required by GDC 2), it has been determined that tube 
    collapse may occur in the steam generators at some plants. This is the 
    case as the tube support plates may become deformed as a result of 
    lateral loads at the wedge supports at the periphery of the plate due 
    to either the LOCA rarefaction wave and/or SSE loadings. Then, the 
    resulting pressure differential on the deformed tubes may cause some of 
    the tubes to collapse.
        There are two issues associated with steam generator tube collapse. 
    First, the collapse of steam generator tubing reduces the RCS [reactor 
    coolant system] flow area through the tubes. The reduction in flow area 
    increases the resistance to flow of steam from the core during a LOCA 
    which, in turn, may potentially increase Peak Clad Temperature (PCT). 
    Second, there is a potential the partial through-wall cracks in tubes 
    could progress to through-wall cracks during tube deformation or 
    collapse or that short through-wall indications would leak at 
    significantly higher leak rates than included in the leak rate 
    assessments.
        Consequently, a detailed leak-before-break analysis was performed 
    and it was concluded that the leak-before-break methodology (as 
    permitted by GDC 4) is applicable to the Farley reactor coolant system 
    primary loops and, thus, the probability of breaks in the primary loop 
    piping is sufficiently low that they need not be considered in the 
    structural design basis of the plant. Excluding breaks in the RCS 
    primary loops, the LOCA loads from the large branch line breaks were 
    analyzed at Farley and were found to be of insufficient magnitude to 
    result in steam generator tube collapse or significant deformation.
        Regardless of whether or not leak-before-break is applied to the 
    primary loop piping at Farley, any flow area reduction is expected to 
    be minimal (much less than 1%) and PCT margin is available to account 
    for this potential effect. Based on analyses' results, no tubes near 
    wedge locations are expected to collapse or deform to the degree that 
    secondary to primary in-leakage would be increased over current 
    expected levels. For all other steam generator tubes, the possibility 
    of secondary-to-primary leakage in the event of a LOCA + SSE event is 
    not significant. In actuality, the amount of secondary-to-primary 
    leakage in the event of a LOCA + SSE is expected to be less than that 
    previously allowed, i.e., 500 gpd per steam generator. Furthermore, 
    secondary-to-primary in-leakage would be less than primary-to-secondary 
    leakage for the same pressure differential since the cracks would tend 
    to tighten under a secondary-to-primary pressure differential. Also, 
    the presence of the tube support plate is expected to reduce the amount 
    of in-leakage.
        Addressing the R.G. 1.83 considerations, implementation of the tube 
    repair criteria is supplemented by 100% inspection requirements at the 
    tube support plate elevations having outside diameter stress corrosion 
    cracking indications, reduced operating leakage limits, eddy current 
    inspection guidelines to provide consistency in voltage normalization, 
    and rotating pancake coil inspection requirements for the larger 
    indications left in service to characterize the principle degradation 
    mechanism as outside diameter stress corrosion cracking.
        As noted previously, implementation of the tube support plate 
    elevation repair criteria will decrease the number of tubes that must 
    be taken out of service with tube plugs or repaired. The installation 
    of steam generator tube plugs or tube sleeves would reduce the RCS flow 
    margin, thus implementation of the voltage-based repair criteria will 
    maintain the margin of flow that would otherwise be reduced through 
    increased tube plugging or sleeving.
        Considering the above, it is concluded that the proposed change 
    does not result in a significant reduction in margin with respect to 
    plant safety as defined in the Final Safety Analysis Report or any 
    bases of the plant Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: William H. Bateman.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
    364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, 
    Alabama
    
        Date of amendments request: January 9, 1995.
        Description of amendments request: The requested changes to the 
    Technical Specifications (TS) would implement the recommended changes 
    from Generic Letter 93-05, ``Line Item Technical Specification 
    Improvements to Reduce Surveillance Requirements for Testing During 
    Power Operation.'' Specifically, the amendments would implement TS 
    changes corresponding to the following GL 93-05 line-item improvement 
    issues: Control Rod Movement Test for Pressurized Water Reactors, 
    Radiation Monitors, Surveillance of Boron Concentration in the 
    Accumulator/Safety Injection/Core Flood Tank, Containment Spray System, 
    Hydrogen Recombiner, and Special Test Exemptions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The proposed changes do not involve any change to the configuration or 
    method [[Page 8757]] of operation of any plant equipment used to 
    mitigate the consequences of an accident. The changes to the 
    surveillance requirements will result in an overall improvement in 
    plant safety by reducing the likelihood of plant trips and subsequent 
    challenges to safety systems, decreasing equipment degradation due to 
    excessive testing, reducing radiation exposure to plant personnel, 
    increasing the availability of safety related equipment, and 
    eliminating an unnecessary burden on plant personnel. Therefore, the 
    proposed changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. The 
    proposed changes do not involve any change to the configuration or 
    method of operation of any plant equipment used to mitigate the 
    consequences of an accident. The relaxation of surveillance tests 
    curtails the excessive amount of testing that increases wear on the 
    equipment and reduces the likelihood of plant trips and subsequent 
    challenges to safety systems. The relaxation also increases the 
    availability of safety related equipment. Accordingly, no new failure 
    modes have been defined for any plant system or component important to 
    safety nor has any new limiting failure been identified as a result of 
    the proposed changes. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed changes do not involve a significant reduction in a 
    margin of safety. The proposed changes eliminate an unnecessary burden 
    without compromising protection for public health and safety. The 
    proposed changes were generically analyzed by the NRC as part of a 
    comprehensive study and presented in NUREG-1366 ``Improvement to 
    Technical specifications (sic) Surveillance Requirements.'' The NRC 
    concluded that while some testing at power is essential to verify 
    equipment and system operability, safety can be improved, equipment 
    degradation decreased, and unnecessary personnel burden relaxed by 
    reducing the amount of testing at power. SNC has analyzed plant 
    operations and made a comparison with the criteria stated in NUREG-1366 
    for the line-item improvements contained in this request and has found 
    the NUREG-1366 basis to be consistent with the Farley design and 
    operation experience. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201.
        NRC Project Director: William H. Bateman.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: December 6, 1994.
        Description of amendment request: The proposed change to Technical 
    Specification 3/4.1.3.2 will delete Surveillance Requirement (SR) 
    4.1.3.2.2, that presently requires, every 31 days, the movement of at 
    least 2% of its height for each Axial Power Shaping Rod not fully 
    withdrawn. The proposed amendment would also change the surveillance 
    intervals for the following Technical Specifications (TS) in accordance 
    with the guidance of Generic Letter 93-05, ``Line Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements For 
    Testing During Power Operation,'' and NUREG-1366, ``Improvements to 
    Technical Specifications Surveillance Requirements:''
        1. TS 4.1.3.2 for the Movable Control Assemblies ``Group Height--
    Safety and Regulating Rod Groups,'' will relax testing requirements 
    from at least once every 31 days to every 92 days.
        2. TS 4.4.6.2, for ``Operational Leakage,'' relaxes the requirement 
    to leakage test RCS pressure isolation valves prior to MODE 2 whenever 
    the plant has been in COLD SHUTDOWN for 72 hours to whenever the plant 
    has been in COLD SHUTDOWN for 7 days.
        3. SR 4.5.2.c.2 for TS 4.5.2, ``ECCS Subsystems--Tavg equal to or 
    greater than 280 deg. F,'' relaxes the inspection requirements for 
    ensuring no debris in containment from ``at the completion of each 
    containment entry'' to ``at least once daily.''
        4. TS 4.6.2.1.d, for the ``Containment Spray System,'' relaxes the 
    SR to perform an air or smoke flow test through the spray header and 
    nozzles from once per 5 years to once per 10 years.
        5. TS 4.10.4.2 for ``Special Test Exceptions Shutdown Margin'' 
    relaxes the SR interval for testing rod insertion capability prior to 
    reducing shutdown margin from 24 hours to 7 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the NRC has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
        (1) The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The change does not involve a significant increase in the 
    probability of an accident previously evaluated nor does it involve a 
    significant increase in the consequences of an accident previously 
    evaluated because no change is being made to any accident initiator and 
    no accident conditions or assumptions used in evaluating the 
    radiological consequences of an accident are changed. Relaxation of 
    surveillance requirements is in accordance with GL 93-05, NUREG-1366, 
    and is compatible with plant operating experience. Deletion of SR 
    4.1.3.2 is consistent with NUREG-1430, ``Improved Standard Technical 
    Specifications for B&W Plants.'' No credit is taken in any accident 
    analysis or mitigation requirements for the Axial Power Shaping Rod 
    Group.
        (2) The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not create the possibility of any new or 
    different kind of accident from any accident previously evaluated 
    because no new accident initiators or assumptions are introduced by 
    these proposed changes. Relaxation of SRs as discussed in GL 93-05 was 
    evaluated as reducing equipment degradation with no increase in safety 
    consequences consistent with the maintenance of plant specific 
    reliability of the equipment and systems affected. Deletion of the SR 
    to move the Axial Power Shaping Rod Group does not affect the 
    requirement to verify rod position, and there is no credit taken for 
    movement of these rods to mitigate an accident.
        (3) The proposed changes do not result in a significant reduction 
    in the margin of safety. [[Page 8758]] 
        The changes do not involve a significant reduction in the margin of 
    safety, because the proposed changes affect only surveillance 
    requirements, do not affect the function of the components and systems 
    involved, and do not decrease the estimated equipment or system 
    reliability.
        Based on the NRC staff analysis, it appears that the three 
    standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: December 6, 1994.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 4.0.5, ``Applicability'' and its 
    associated Bases; TS 3/4.1.2.3, ``Reactivity Control Systems--Makeup 
    Pump--Shutdown; TS 3/4.1.2.4, ``Reactivity Control Systems--Makeup 
    Pump--Operating; TS 3/4.1.2.6, Reactivity Control Systems--Boric Acid 
    Pump--Shutdown; and TS 3/4.1.2.7, ``Reactivity Control System--Boric 
    Acid Pumps--Operating.'' The proposed change would replace the specific 
    monthly surveillance requirements associated with the makeup pumps and 
    boric acid pumps with a surveillance requirement referencing TS 4.0.5, 
    which references Section XI of the American Society of Mechanical 
    Engineers Boiler and Pressure Vessel Code for quarterly pump testing 
    requirements. The proposed change to TS 4.0.5 and its associated Bases 
    would revise the requirement regarding the NRC's approval of relief 
    requests to be in accordance with the NRC Staff's recommendation 
    contained in NUREG-1482, ``Guidelines for Inservice Testing at Nuclear 
    Power Plants.'' Additionally, TS 4.0.5.a.2 which describes historical 
    requirements for inservice inspection and testing would be deleted and 
    TS 4.0.5.a.1 would be renumbered as TS 4.0.5.a.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the NRC Staff has 
    performed an analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Operation of the Davis-Besse Nuclear Power Station, Unit No. 1, in 
    accordance with these changes, would not involve a significant increase 
    in the probability of an accident previously evaluated because no 
    accident initiators, conditions, or assumptions are affected by the 
    proposed changes to replace the specific monthly surveillance 
    requirements for the makeup and boric acid pumps with surveillance 
    requirements referencing TS 4.0.5 (ASME Boiler and Pressure Vessel Code 
    Section XI requirements) and to delete wording regarding NRC approval 
    of relief requests. The changes do not involve a significant increase 
    in the consequences of an accident previously evaluated, because no 
    accident conditions or assumptions are affected that would increase the 
    radiological consequences of a previously evaluated accident.
        (2) The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not result in any new accident initiators 
    nor do they alter any accident scenarios. The changes do not create the 
    possibility of a different kind of accident from any accident 
    previously evaluated, because the surveillance requirements for the 
    makeup and boric acid pumps only affect the testing of existing 
    components, systems, and functions, and do not introduce any new 
    requirements.
        (3) The proposed changes do not result in a significant reduction 
    in the margin of safety.
        The proposed changes do not reduce or adversely affect the 
    capabilities or reliability of any plant structures, systems or 
    components. Relaxation of the surveillance testing interval for the 
    boric acid and makeup pumps and modifying the testing requirements is 
    consistent with previous NRC guidance.
        Based on this NRC staff evaluation, it appears that the three 
    standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: January 13, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) by relocating Tables 3.3-2, 
    ``Reactor Trip System Instrumentation Response Times,'' and 3.3-5, 
    ``Engineered Safety Features Response Times,'' to FSAR Chapter 16, 
    Section 16.3. The Bases discussion specific to Table 3.3-5 would also 
    be relocated to FSAR Section 16.3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed revision does not involve a significant hazards 
    consideration because operation of Callaway Plant with this change 
    would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Overall protection system performance will remain within the bounds 
    of the accident analyses documented in FSAR Chapter 15, WCAP-10961-P, 
    and WCAP-11883 since no changes to the response times or measurement 
    interval are proposed.
        The RTS and ESFAS will continue to function in a manner consistent 
    with the above analysis assumptions and the plant design basis. As 
    such, there will be no degradation in the performance of nor an 
    increase in the number of challenges to equipment assumed to function 
    during an accident situation.
        These Technical Specification revisions do not involve any hardware 
    changes nor do they affect the probability of any event initiators. 
    There will be no change to normal plant operating parameters or 
    accident mitigation capabilities. Therefore, there will be no increase 
    in the probability or consequences of any accident occurring due to 
    these changes.
        (2) Create the possibility of a new or different kind of accident 
    from any previously evaluated. [[Page 8759]] 
        As discussed above, there are no hardware changes associated with 
    these Technical Specification revisions nor are there any changes in 
    the method by which any safety-related plant system performs its safety 
    function. The normal manner of plant operation is unaffected.
        No new accident scenarios, transient precursors, failure 
    mechanisms, or limiting single failures are introduced as a result of 
    these changes. There will be no adverse effect or challenges imposed on 
    any safety-related system as a result of these changes. Therefore, the 
    possibility of a new or different type of accident is not created.
        (3) Involve a significant reduction in a margin of safety.
        No response time changes are proposed in this amendment 
    application; only the document where these limits are listed will be 
    changed. There will be no effect on the manner in which safety limits 
    or limiting safety system settings are determined nor will there be any 
    effect on those plant systems necessary to assure the accomplishment of 
    protection functions. There will be no impact on DNBR limits, FQ, 
    F-delta-H, LOCA PCT, peak local power density, or any other margin of 
    safety.
        Based upon the preceding information, it has been determined that 
    the proposed changes to the Technical Specifications do not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated, create the possibility of a new or different kind 
    of accident from any accident previously evaluated, or involve a 
    significant reduction in a margin of safety. Therefore, it is concluded 
    that the proposed changes meet the requirements of 10CFR50.92(C) [sic] 
    and do not involve a significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: December 8, 1994.
        Description of amendment request: The proposed amendment would 
    change Standby Gas Treatment Power Supply Requirements during refueling 
    operations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    SGTS [Standby Gas Treatment System] DURING REFUELING OPERATIONS 
    (Specification 3.7.B.1, 3.7.B.3)
        1. The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously evaluated. 
    The Standby Gas Treatment System (SGTS) is not the initiator of any 
    accident. SGTS may be required to operate for a design basis loss of 
    coolant accident or for a refueling accident in order to mitigate the 
    consequences of said accident by providing a filtered exhaust path to 
    minimize the potential release of radioactive material to the environs. 
    The proposed amendment does not reduce or change the operational 
    requirements for the SGTS for an accident. The proposed amendment now 
    clearly defines the operability requirements during refueling 
    conditions. The proposed amendment further requires the availability of 
    a second auxiliary power supply in the event that an Emergency Diesel 
    Generator (EDG) is out of service during refueling operations, not 
    currently required. We conclude, therefore, that the proposed amendment 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously evaluated. 
    The SGTS is not an accident initiator, therefore, the proposed 
    amendment will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed amendment will not involve a significant reduction 
    in a margin of safety. The proposed amendment requires the availability 
    of a second auxiliary power supply in the event that an EDG is out of 
    service during refueling operations, not currently required. 
    Maintaining availability of a specific reliable auxiliary electrical 
    power source as an alternative to an EDG in this mode provides 
    assurance that SGTS can, if required, be operated without placing undue 
    constraints on EDG availability and represents an enhancement that 
    increases a margin of safety. We conclude, therefore, that the proposed 
    amendment does not involve a significant reduction in a margin of 
    safety.
        Based on the above discussion, we have determined that this change 
    does not constitute a significant hazards consideration as defined in 
    10CFR50.92(c).
    LABORATORY CARBON SAMPLE ANALYSIS (Specification 3.7.B.2.b)
        1. The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously evaluated. 
    The Standby Gas Treatment System (SGTS) is not the initiator of any 
    accident. SGTS may be required to operate for a design basis loss of 
    coolant accident or for a refueling accident in order to mitigate the 
    consequences of said accident by providing a filtered exhaust path to 
    minimize the potential release of radioactive material to the environs. 
    The proposed amendment does not reduce or change the operational 
    requirements for the SGTS for an accident. The proposed amendment now 
    clearly defines the operability requirements during the interval 
    between sample removal and completion of laboratory analysis.
        2. The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously evaluated. 
    The SGTS is not an accident initiator, therefore, the proposed 
    amendment will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed amendment will not involve a significant reduction 
    in a margin of safety. The proposed change does not reduce the 
    requirements or acceptance criteria for sampling, testing or analysis. 
    The proposed change only incorporates into the specification an 
    existing clarification which addresses the determination of operability 
    during the time between sample removal and completion of laboratory 
    analysis. The change provides an explicit time limit consistent with 
    current regulatory criteria for completion of analyses.
        Based on the above discussion, we have determined that this change 
    does not constitute a significant hazards [[Page 8760]] consideration 
    as defined in 10CFR50.92(c).
    TORUS VENT MODE (Specification 4.7 B.2.c)
        1. The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously evaluated. 
    The Standby Gas Treatment System (SGTS) is not the initiator of any 
    accident. SGTS may be required to operate for a design basis loss of 
    coolant accident or for a refueling accident in order to mitigate the 
    consequences of said accident by providing a filtered exhaust path to 
    minimize the potential release of radioactive material to the environs. 
    The proposed amendment does not reduce or change the operational 
    requirements for the SGTS for an accident.
        2. The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously evaluated. 
    The SGTS is not an accident initiator, therefore, the proposed 
    amendment will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed amendment will not involve a significant reduction 
    in a margin of safety. The proposed change will incorporate into the 
    specification an existing clarification. Use of the SGTS filters during 
    Torus venting results in an insignificant flow through the filters. 
    Further, maintaining humidity control prevents any adsorber 
    degradation. Past sample testing on a six month calendar interval when 
    720 hours operating time has not accumulated has shown no detectable 
    impact.
        Based on the above discussion, we have determined that this change 
    does not constitute a significant hazards consideration as defined in 
    10CFR50.92(c).
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, Vermont 05301.
        Attorney for licensee: John A. Ritsher, Esquire, Ropes and Gray, 
    One International Place, Boston, Massachusetts 02110-2624.
        NRC Project Director: Walter R. Butler.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: November 19, 1994.
        Brief description of amendment: The proposed amendment would revise 
    Section 3.10.8 and the associated Bases of the Indian Point Nuclear 
    Generating Unit No. 3 Technical Specifications. Specifically, the 
    proposed revision would reduce the maximum allowable control rod drop 
    time from 2.4 to 1.8 seconds. The change would remove, for testing 
    purposes, the allowance for a seismic event (0.6 seconds), which had 
    been integral to the 2.4 second safety analysis basis. Since a seismic 
    event cannot be simulated during the rod drop time test, the more 
    conservative testing acceptance criteria value of 1.8 seconds is needed 
    to ensure that the plant is within its design basis. This proposed 
    revision will support control rod testing which is required during 
    startup from the current outage.
        Date of publication of individual notice in Federal Register: 
    January 20, 1995 (60 FR 4203).
        Expiration date of individual notice: February 21, 1995.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units 1, 2, 
    and 3, Maricopa County, Arizona
    
        Date of application for amendments: November 30, 1994.
        Brief description of amendments: These amendments relocate Table 
    3.3-2, ``Reactor Protective Instrumentation Response Times,'' and Table 
    3.3-5, ``Engineered Safety Features Response Times,'' of TS 3/4.3.1 and 
    3/4.3.2, respectively, to the Palo Verde Updated Final Safety Analysis 
    Report (UFSAR) in accordance with the guidance provided in Generic 
    Letter 93-08. In addition, the amendments make administrative changes 
    to two previous TS amendment requests to maintain consistency with the 
    deletion of Tables 3.3-2 and 3.3-5. The amendments also delete an 
    obsolete footnote on page 3/4 3-17 of the Palo Verde Unit 2's TS. 
    [[Page 8761]] 
        Date of issuance: February 3, 1995.
        Effective date: February 3, 1995.
        Amendment Nos.: 88, 75 and 59.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    496) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 3, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of application for amendments: November 16, 1994.
        Brief description of amendments: The proposed amendments change the 
    Technical Specifications to revise the wording for the containment 
    integrated leakage rate testing in Section 3/4.6.1.2 to make it 
    consistent with the requirements of the BWR-4 Improved Standard 
    Technical Specifications (NUREG-1433).
        Date of issuance: January 26, 1995.
        Effective date: January 26, 1995.
        Amendment Nos.: 173 and 204.
        Facility Operating License Nos. DPR-71 and DPR-62.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65810).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated January 26, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. STN 
    50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: June 13, 1994, as supplemented 
    on October 7, 1994.
        Brief description of amendments: The amendments revise the 
    administrative controls in Section 6 of the technical specifications 
    (TS). The changes include: (1) a change to the submittal frequency of 
    the Radiological Effluent Release Report from semiannually to annually; 
    (2) changes to the Shift Technical Advisor (STA) description; (3) a 
    clarification of the Shift Engineer responsibilities; and (4) several 
    editorial changes.
        Date of issuance: February 2, 1995.
        Effective date: February 2, 1995.
        Amendment Nos.: 69, 69, 59 and 59.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: October 26, 1994 (59 FR 
    53839).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    
        Date of application for amendment: May 17, 1993 as supplemented 
    October 12, 1994.
        Brief description of amendment: The amendment replaces License 
    Condition 2.C.4, relating to the implementation and maintenance of the 
    approved Fire Protection Program, in its entirety with a new License 
    Condition. In conjunction, with this change, and in accordance with GL 
    86-10, Technical Specification provisions related to the Fire 
    Protection Program are being deleted and placed in the Updated Final 
    Safety Analysis Report.
        Date of Issuance: February 1, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 179.
        Facility Operating License No. DPR-61. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36432).
        The October 12, 1994, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated February 1, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina Date of 
    application for amendments: August 25, 1994, as supplemented November 
    16, 1994.
    
        Brief description of amendments: The amendments revise Technical 
    Specification Table 3.3-4, by revising the ``Trip Setpoint'' and 
    ``Allowable Value'' for the 4 kV bus undervoltage grid degraded voltage 
    relays and the ``Allowable Value'' for the 4 kV undervoltage loss of 
    voltage/loss of offsite power relays. This revision was submitted in 
    response to a concern identified by the licensee in their Self-
    Initiated Technical Audit and during the electrical distribution system 
    functional inspection team findings.
        Date of issuance: January 20, 1995.
        Effective date: To be implemented within 30 days from the date of 
    issuance.
        Amendment Nos.: 127 and 121.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 12, 1994 (59 FR 
    51619).
        The November 16, 1994, letter provided clarifying information that 
    did not change the scope of the August 25, 1994, application and the 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated January 20, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Florida Power and Light Company, Docket No. 50-335, St. Lucie Plant, 
    Unit No. 1, St. Lucie County, Florida
    
        Date of application for amendment: July 28, 1994.
        Brief description of amendment: This amendment revises Technical 
    Specifications 3/4.4.13 to incorporate Low Temperature Overpressure 
    Protection requirements similar to those recommended by the NRC staff 
    via Generic Letter 90-06. [[Page 8762]] 
        Date of Issuance: January 27, 1995.
        Effective Date: January 27, 1995.
        Amendment No.: 132.
        Facility Operating License No. DPR-67: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42341).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 27, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of application for amendments: February 3, 1994.
        Brief description of amendments: The amendments relocate the 
    requirements of Technical Specification 3/4.7.10, Area Temperature 
    Monitoring, to section 16.3 of the VEGP Final Safety Analysis Report 
    (FSAR). With this relocation to the FSAR, GPC plans to clarify the 
    basis for areas to be monitored and modify these surveillance 
    requirements. This change is in accordance with NUREG-1431, ``Standard 
    Technical Specifications, Westinghouse Plants.''
        Date of issuance: January 23, 1995.
        Effective date: To be implemented within 30 days from the date of 
    issuance.
        Amendment Nos.: 83 and 61.
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 2, 1994 (59 
    FR 45735).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated January 23, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: May 13, 1992.
        Brief description of amendment: The amendment changes the allowable 
    primary-to-secondary leakage rate, as specified in License Condition 
    2.c.(8)2, from 0.1 gallons per minute (gpm) to 0.2 gpm.
        Date of Issuance: January 31, 1995.
        Effective date: January 31, 1995.
        Amendment No.: 193.
        Facility Operating License No. DPR-50. Amendment revises a License 
    Condition.
        Date of initial notice in Federal Register: October 14, 1992 (57 FR 
    47137).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated January 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: September 26, 1994.
        Brief description of amendment: The amendment revised Technical 
    Specification 3.5.C.1 and 3.5.C.4 to increase the minimum pressure at 
    which the high pressure coolant injection system is required to be 
    operable from 113 psig to 150 psig.
        Date of issuance: January 25, 1995.
        Effective date: January 25, 1995.
        Amendment No.: 166.
        Facility Operating License No. DPR-46. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 26, 1994 (59 FR 
    53841). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated January 25, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Auburn Public Library, 118 
    15th Street, Auburn, Nebraska 68305.
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: December 22, 1994.
        Brief description of amendment: The amendment revised Technical 
    Specification 1.0.J, definition of limiting conditions for operation, 
    consistent with the guidance provided in NRC Generic Letter 87-09, 
    ``Sections 3.0 and 4.0 of the Standard Technical Specifications on the 
    Applicability of Limiting Conditions for Operation and Surveillance 
    Requirements.''
        Date of issuance: February 3, 1995.
        Effective date: February 3, 1995.
        Amendment No.: 168.
        Facility Operating License No. DPR-46. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1995 (60 FR 
    153).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 3, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Auburn Public Library, 118 
    15th Street, Auburn, Nebraska 68305.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York.
    
        Date of application for amendment: July 21, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specifications 2.2.2, 3.2.8, 4.2.8, and the associated Bases to reduce 
    the number of reactor head safety valves required operable from 16 
    valves to 9 valves. The setpoints of the valve groups are unchanged by 
    this amendment. The amendment requires testing of the safety valves in 
    accordance with the approved NMP-1 Inservice Test Program.
        Date of issuance: January 25, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 152.
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45027).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 25, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point
    
        Nuclear Station, Unit 2, Oswego County, New York.
        Date of application for amendment: October 28, 1994.
        Brief description of amendment: The amendment revises Technical 
    [[Page 8763]] Specification (TS) 1.7, ``CORE ALTERATION,'' to state 
    that movement or replacement of incore instrumentation is not 
    considered to be a CORE ALTERATION and that movement of control rods is 
    not considered a CORE ALTERATION provided there are no fuel assemblies 
    in the associated core cell. This amendment includes changes to TS 3/
    4.9.3, ``Control Rod Position,'' and associated Bases to be consistent 
    with the revision to TS 1.7. TS 3/4.9.3 is being revised to require 
    that all control rods be inserted only during loading of fuel 
    assemblies into the core rather than during CORE ALTERATIONS. These 
    changes are consistent with the NRC's, ``Improved Standard Technical 
    Specifications,'' (NUREG-1434).
        This amendment also revises Item 1.i.3) of TS Tables 3.3.2-1 and 
    4.3.2.1-1 to delete the requirement for Reactor Water Cleanup isolation 
    due to actuation of the Standby Liquid Control System (SLCS) in 
    OPERATIONAL CONDITION 5. License Amendment No. 48 issued on September 
    30, 1993, deleted the requirement for the SLCS to be OPERABLE in 
    OPERATIONAL CONDITION 5; however, due to an oversight, Item 1.i.3) and 
    associated notations were not deleted from TS Tables 3.3.2-1 and 
    4.3.2.1-1 as part of License Amendment No. 48. This amendment corrects 
    that oversight.
        Date of issuance: January 20, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 61.
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 23, 1994 (59 
    FR 60382).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 20, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: November 14, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specification 4.5.1.e.2.e) to reduce the leak rate test pressure for 
    the Automatic Depressurization System (ADS) nitrogen receiving tanks 
    from 385 psig to 365 psig.
        Date of issuance: January 31, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 62.
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65817).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: January 14, 1994, as modified by letter 
    dated October 17, 1994.
        Description of amendment request: The amendment revises the 
    Appendix A Technical Specifications (TS) to specify the composition of 
    the Station Operation Review Committee (SORC) based on experience and 
    expertise vice organizational position, to implement a Station 
    Qualified Reviewer Program (SQRP), and to revise the time within which 
    the Nuclear Safety Audit Review Committee (NSARC) must issue reports 
    and minutes.
        The amendment also incorporated a number of editorial changes to 
    delete certain items that are no longer applicable; remove 
    inconsistencies involving the names of systems, equipment and NSARC 
    function, composition, and use of alternates; and correct the value for 
    the reactor coolant system volume. Other editorial changes have been 
    incorporated for document format consistency. The amendment affects the 
    following: TS Sections 1.31, 3.3.3.6, 3.4.1.2, 4.6.3.2, 3.7.1.2, 3/4 
    10.6, 5.4.2, 6.3.1, 6.4, 6.7, and 6.8.1.4, and Table 4.3-1.
        Date of issuance: January 26, 1995.
        Effective date: January 26, 1995.
        Amendment No.: 34.
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27057) The licensee's letter dated October 17, 1994, provided 
    clarification and minor revision to the application but does not change 
    the initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated January 26, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 47 
    Front Street, Exeter, NH 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of application for amendment: July 22, 1994.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to incorporate a different setpoint and transient 
    methodology for determining the maximum allowable power range neutron 
    flux setpoint. These changes allow Millstone Unit 3 to operate with a 
    reduced number of main steam-line safety valves at a reduced power 
    level, as determined by the high flux setpoint.
        Date of issuance: January 31, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 102.
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47171).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: October 25, 1994.
        Brief description of amendments: These amendments add to the 
    Susquehanna, Units 1 and 2, Technical Specifications, isolation signals 
    to Table 3.6.3-1 for the containment isolation valves on the sample 
    lines for the containment radiation monitoring and 
    [[Page 8764]] wetwell sample lines. This change is based on the 
    licensee's design change for installation of a new CRM and wetwell 
    sample system.
        Date of issuance: January 31, 1995.
        Effective date: January 31, 1995.
        Amendment Nos.: 141 and 111.
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63126). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 31, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick Generating 
    Station, Unit 1, Montgomery County, Pennsylvania.
    
        Date of application for amendment: June 10, 1994, as supplemented 
    by letter dated December 19, 1994.
        Brief description of amendment: This amendment involves a one-time 
    change affecting the Allowed Outage Time (AOT) for the Emergency Sevice 
    Water (ESW) system, Residual Heat Removal Service Water (RHRSW) System, 
    the Suppression Pool Cooling, the Suppression Pool Spray, and Low 
    Pressure Coolant Injection modes of the Residual Heat Removal System, 
    and Core Spray System to be extended from 3 and 7 days to 14 days 
    during the Unit 2 refueling outage scheduled to begin in January 1995. 
    This proposed extended AOT allows adequate time to install isolation 
    valves and cross-ties on the ESW and RHRSW Systems to facilitate future 
    inspections or maintenance.
        Date of issuance: January 27, 1995.
        Effective date: January 27, 1995.
        Amendment No. 86.
        Facility Operating License No. NPF-39. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37077). The December 19, 1994 letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 27, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket No. 50-353, Limerick Generating 
    Station, Unit 2, Montgomery County, Pennsylvania
    
        Date of application for amendment: June 30, 1994.
        Brief description of amendment: This amendment removes the controls 
    for a remote shutdown system control valve and the primary containment 
    isolation valves from TS Tables 3.3.7.4-1 and 3.6.3-1 respectively, as 
    a result of eliminating the steam condensing mode of the Residual Heat 
    Removal system.
        Date of issuance: January 27, 1995.
        Effective date: January 27, 1995.
        Amendment No. 47.
        Facility Operating License No. NPF-85. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42343).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 27, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket No. 50-353, Limerick Generating 
    Station, Unit 2, Montgomery County, Pennsylvania
    
        Date of application for amendment: August 27, 1993, supplemented by 
    letter dated November 17, 1993.
        Brief description of amendment: The amendment allows an expanded 
    operating domain for the Limerick Generating Station (LGS), Unit 2, 
    resulting from the implementation of the Average Power Range Monitor--
    Rod Block Monitor Technical Specifications/Maximum Extended Load Line 
    Limit Analysis. These improvements are a prerequisite for Power Rerate 
    Program implementation at Limerick Generating Station, Unit 2.
        Date of issuance: January 27, 1995.
        Effective date: January 27, 1995.
        Amendment No. 48.
        Facility Operating License No. NPF-85. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 13, 1993 (58 FR 
    52992). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 27, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: August 22, 1994.
        Brief description of amendments: These amendments revise TS 3.1.5, 
    ``Standby Liquid Control System,'' to remove the requirement for the 
    standby liquid control system to be operable in OPERATIONAL CONDITION 
    5, Refueling, when any control rod is withdrawn and the TS definition 
    of CORE ALTERATION to exclude control rod movement in a control cell 
    that contains no fuel assemblies.
        Date of issuance: January 27, 1995.
        Effective date: January 27, 1995.
        Amendment Nos. 87/49.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55881).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated January 27, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: September 28, 1993.
        Brief description of amendment: The amendment revised Technical 
    Specification (TS) Section 4.11.D to change the surveillance 
    requirements for the Emergency Service Water System pumps. The change 
    added pump flow rate requirements and tests the pumps in accordance 
    with the licensee's Inservice Testing Program. The respective TS Bases 
    were also revised.
        Date of issuance: January 30, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 223.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1993 (58 
    FR 62156). [[Page 8765]] 
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 30, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: January 3, 1995 (TS 95-01).
        Brief description of amendments: The amendments add a permissive 
    statement to Surveillance Requirement 4.9.7.1 that will allow the 
    auxiliary building bridge crane interlocks and physical stops to be 
    defeated during implementation of the spent fuel pool storage capacity 
    increase modification.
        Date of issuance: January 24, 1995.
        Effective date: January 24, 1995.
        Amendment Nos.: 194 and 185.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: January 9, 1995 (60 FR 
    2404) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated January 24, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration amd 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By March 17, 1995, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted [[Page 8766]] with particular 
    reference to the following factors: (1) the nature of the petitioner's 
    right under the Act to be made a party to the proceeding; (2) the 
    nature and extent of the petitioner's property, financial, or other 
    interest in the proceeding; and (3) the possible effect of any order 
    which may be entered in the proceeding on the petitioner's interest. 
    The petition should also identify the specific aspect(s) of the subject 
    matter of the proceeding as to which petitioner wishes to intervene. 
    Any person who has filed a petition for leave to intervene or who has 
    been admitted as a party may amend the petition without requesting 
    leave of the Board up to 15 days prior to the first prehearing 
    conference scheduled in the proceeding, but such an amended petition 
    must satisfy the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: July 26, 1994, as supplemented by 
    letters dated December 27, 1994, and January 27, 1995.
        Brief description of amendment: The amendment changed the Technical 
    Specification Section 3/4.12.A to allow for increased flow capacity of 
    the control room emergency filter system. By increasing the maximum 
    allowed makeup capacity of this system, additional margin is provided 
    for the positive pressurization of the control room envelope.
        Date of issuance: January 27, 1995.
        Effective date: January 27, 1995.
        Amendment No.: 167.
        Facility Operating License No. DPR-46. Amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated
        Local Public Document Room location: Auburn Public Library, 118 
    15th Street, Auburn, Nebraska 68305.
        Attorney for licensee: Mr. G.D. Watson, Nebraska Public Power 
    District, Post Office Box 499, Columbus, Nebraska 68602-0499.
        NRC Project Director: William D. Beckner.
    
        Dated at Rockville, Maryland, this 8th day of February 1995.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Deputy Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 95-3629 Filed 2-14-95; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Effective Date:
2/3/1995
Published:
02/15/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-3629
Dates:
February 3, 1995.
Pages:
8741-8766 (26 pages)
PDF File:
95-3629.pdf