99-4391. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 36 (Wednesday, February 24, 1999)]
    [Notices]
    [Pages 9183-9209]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-4391]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from January 30, 1999, through February 11, 1999. 
    The last biweekly notice was published on February 10, 1999.
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By March 26, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
    
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        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: January 28, 1999.
        Description of amendment request: The H. B. Robinson, Unit No. 2, 
    Technical Specifications (TSs) are proposed to be changed to replace 
    and add analytical methodologies used to determine acceptable core 
    designs and provide inputs to methodologies that develop the core 
    operating limits in the Core Operating Limits Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes in a methodology have been previously 
    generically reviewed and approved for use by the NRC for determining 
    core neutronics design and gadolinimum oxide thermal conductivity. 
    Analyzed events are assumed to be initiated by the failure of plant 
    structures, systems, or components. The fuel design parameters 
    developed in accordance with the new methodologies are bounded by 
    the limitations in the NRC acceptance in its safety evaluations of 
    the new methodologies. The topical reports associated with the new 
    methodologies demonstrate that the integrity of the fuel will be 
    maintained during normal operations and that design requirements 
    preclude fuel rods containing gadolinium oxide from being limiting 
    in accident and related safety analyses. The proposed change does 
    not have a detrimental impact on the integrity of any plant 
    structure, system, or component. The proposed change will not alter 
    the operation of any plant equipment, or otherwise increase its 
    failure probability. Therefore, the probability of occurrence for a 
    previously analyzed accident is not significantly increased.
        The consequences of a previously analyzed accident are dependent 
    on the initial conditions assumed for the analysis, the behavior of 
    the fuel during the analyzed accident, the availability and 
    successful functioning of the equipment assumed to operate in 
    response to the analyzed event, and the setpoints at which these 
    actions are initiated. The proposed changes to methodology continues 
    to meet applicable design and safety analyses acceptance criteria 
    for neutronics design analysis and gadolinimum oxide thermal 
    conductivity. The topical reports associated with the new 
    methodologies demonstrate that the integrity of the fuel will be 
    maintained as is assumed or is bounded initially in accident 
    analyses and that design requirements preclude fuel rods containing 
    gadolinimum oxide from being limiting in accident and related safety 
    analyses. The proposed change does not affect the performance of any 
    equipment used to mitigate the consequences of an analyzed accident. 
    As a result, no analyses assumptions are violated and there are no 
    adverse effects on the factors that contribute to offsite or onsite 
    dose as the result of an accident. The proposed change does not 
    affect setpoints that initiate protective or mitigative actions. The 
    proposed change ensures that plant structures, systems, or 
    components are maintained consistent with the safety analysis and 
    licensing bases. Based on this evaluation, there is no significant 
    increase in the consequences of a previously analyzed event.
        Therefore, the proposed change does not involve any increase in 
    the probability or consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not involve any physical alteration of 
    plant systems, structures, or components. The proposed changes in 
    methodology continue to meet applicable criteria for neutronics 
    design analysis and assure that design requirements preclude fuel 
    rods containing gadolinimum oxide from being limiting. The proposed 
    change does not involve a physical alteration of the plant other 
    than allowing for fuel design in accordance with NRC approved 
    methodologies. No new or different equipment is being installed. No 
    installed equipment is being operated in a different manner. There 
    is no alteration to the parameters within which the plant is 
    normally operated or in the setpoints that initiate protective or 
    mitigative actions. As a result no new failure modes are being 
    introduced. There are no changes in the methods governing normal 
    plant operation, nor are the methods utilized to respond to plant 
    transients altered. Therefore, the proposed change does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The margin of safety is established through the design of the 
    plant structures, systems, and components, through the parameters 
    within which the plant is operated, through the establishment of the 
    setpoints for the actuation of equipment relied upon to respond to 
    an event, and through margins contained within the safety analyses. 
    The proposed change is to methodologies that continue to meet 
    applicable criteria for neutronics design analysis and continues to 
    assure that design requirements preclude fuel rods containing 
    gadolinimum oxide from being limiting. The proposed change does not 
    impact the condition or performance of structures, systems, 
    setpoints, and components relied upon for accident mitigation. The 
    proposed change does not significantly impact any safety analysis 
    assumptions or results. Therefore, the proposed change does not 
    result in a significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
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        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Cecil B. Thomas.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of amendment request: November 25, 1998.
        Description of amendment request: The proposed amendments would 
    revise Improved Technical Specifications 3.8.4 and 3.8.9 to support on-
    line replacement of the Braidwood 125 Volt DC AT&T batteries with new 
    Charter Systems Inc. batteries.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        During the replacement of the existing batteries, a temporary 
    battery bank will provide the same function as the AT&T batteries 
    being removed. Even though this temporary battery will not be 
    seismically mounted, due to its location in the Turbine Building, it 
    is the safety related AT&T battery which was previously qualified 
    and used to perform this function on Unit 1.
        While the temporary battery is being connected, the DC bus will 
    be supplied by the existing crosstie with Unit 1. Similar crosstie 
    conditions are allowed under the present Improved Technical 
    Specifications.
        The DC system is normally supplied by the AC system through the 
    ESF [Engineered Safety Feature] battery charger. The essential 
    function of the DC system battery is to supply control power 
    necessary to start and load the Diesel Generators. Once the Diesel 
    Generators are on line, the DC system will be supplied via the 
    battery charger. However, the ESF batteries have been sized for one 
    hour to provide additional assurance that the critical DC loads are 
    available in the event of a loss of a battery charger.
        During the 10 day Completion Time when the temporary battery and 
    the ESF charger are supporting the bus, the ability of that DC 
    Division to mitigate an event/accident is unchanged except for its 
    ability to cope with a seismic event. However, the probability of a 
    seismic event concurrent with the 10 day Completion Time is 
    extremely small. During a seismic event, one DC division may be 
    compromised, however, the unit has adequate DC power available in 
    the form of the other division to mitigate all Design Basis 
    accidents. This loss of one DC division is bounded by the loss of an 
    entire AC division, a condition which the plant is currently 
    evaluated to withstand.
        During the 8 hour Completion Time to connect and disconnect the 
    temporary battery, there is no adverse impact on Unit 1. The 
    compensatory measures to manually open the crosstie will ensure the 
    Unit 1 DC battery can supply its required loads for the entire one 
    hour duty cycle. The Unit 2 DC bus, which is crosstied, will be de-
    energized in the event of a Unit 2 accident based on the 
    compensatory measures. This action would only be required if the 
    associated Diesel Generator were to fail to re-energize its 
    associated charger. This condition is consistent with the other 
    crosstie scenarios currently permitted by the Technical 
    Specifications. Thus, the 8 hour Completion Time is consistent with 
    the two hour Completion Time with respect to the ability to safely 
    shutdown the Unit. Only the duration of the Completion Time is 
    different.
        Based on the above, the overall design, function, and operation 
    of the DC system and equipment has not been significantly modified 
    by these changes. The proposed changes do not affect any accident 
    initiators or precursors and do not alter the design assumptions for 
    the systems or components used to mitigate the consequences of an 
    accident as analyzed in UFSAR Chapter 15.
        Therefore, this proposed amendment does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        During the replacement of the existing batteries, a temporary 
    battery bank will provide the same function as the batteries being 
    removed. Even though this temporary battery is not seismically 
    mounted, it is the safety related AT&T battery which was previously 
    qualified and utilized to perform this function on Unit 1. Because 
    this temporary battery is identical to the battery that is currently 
    installed, and will be connected and used in the same way, no new 
    electrical or functional failure modes are created.
        The temporary battery will be located in the turbine building, 
    which is non-seismic. The temporary battery will not be seismically 
    mounted. Thus, a seismic failure of the batteries is possible. Since 
    the temporary battery is located in the turbine building the 
    potential for battery failure to initiate an accident is not 
    present, and failure of the battery cannot create a different 
    response from any previously postulated accident.
        Due to the location of the main generator in relationship to the 
    temporary batteries, a turbine blade failure would not hit the 
    battery unless it penetrated the turbine casing and ricocheted in 
    the direction of the battery, which is an unlikely scenario due to 
    the orientation of the temporary battery. Likewise, an unmitigated 
    Outside Containment Steam Line Break of either unit would be 
    interrupted by the successful closure of all MSIVs [Main Steam 
    Isolation Valves] thereby leaving the battery and the DC bus intact 
    and available. Also any affects of a postulated storm on the turbine 
    building have been previously addressed and would not change as a 
    result of the batteries being temporary located there.
        While the temporary battery is being connected, the DC bus will 
    be supplied by the existing crosstie with Unit 1. To prevent any 
    occurrence on Unit 2 from adversely affecting Unit 1, this crosstie 
    will be manually disconnected based on specific criteria that may be 
    indicative of a Unit 2 accident (specifically a Unit 2 LOOP). Once 
    the crosstie is opened, the Unit 2 bus will be de-energized and the 
    other Unit 2 division will be required to mitigate the accident. 
    This loss of one DC division is bounded by the loss of one division 
    (AC or DC), a condition which the plant is currently evaluated to 
    withstand.
        The DC system and its equipment will continue to perform the 
    same function and be operated in the same fashion. The proposed 
    changes do not introduce any new accident initiators or precursors, 
    or any new design assumptions for the systems or components used to 
    mitigate the consequences of an accident. Therefore, the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated has not been created.
        Therefore, this proposed amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Does the change involve a significant reduction in a margin of 
    safety?
        During the replacement of the existing batteries, a temporary 
    safety related battery bank will perform the same function as the 
    batteries being removed. Even though this temporary battery is not 
    seismically mounted, it is the safety related battery which was 
    previously qualified and used to perform this function on Unit 1 and 
    is identical to the safety related battery that is currently 
    installed. Therefore, it has the same capacity, margin and 
    capability to fulfill the requirements of the Unit 2 DC bus as the 
    existing qualified battery. The proposed replacement activity will 
    not prevent the plant from responding to either a seismic event or 
    design basis accident. In both cases, the design mitigation 
    capability will be maintained. Due to the limited duration of the 
    activity and the planned contingency actions, a significant 
    reduction in the margin of safety will not result.
        While the temporary battery is being connected, the DC bus will 
    be supplied by the existing crosstie with Unit 1. This condition is 
    currently allowed for a limited time by the Improved Technical 
    Specifications.
        The inherent design conservatism of the DC system and its 
    equipment has not been altered. The DC system and its equipment will 
    continue to be operated with the same degree of conservatism. 
    Accordingly, there is no significant reduction in the margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are
    
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    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Wilmington Public Library, 201 
    S. Kankakee Street, Wilmington, Illinois 60481.
        Attorney for licensee: Ms. Pamela B. Stroebel, Senior Vice 
    President and General Counsel, Commonwealth Edison Company, P.O. Box 
    767, Chicago, Illinois 60690-0767.
        NRC Project Director: Stuart A. Richards.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois; Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of amendment request: December 29, 1998.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specification Tables 3.3.1-1 and 3.3.2-1, to 
    revise twelve Reactor Trip System and Engineered Safety Feature 
    Actuation System Allowable Values.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        These changes to the twelve AVs [Allowable Values] do not 
    involve an increase in the probability of an accident previously 
    evaluated. The AVs provide the basis for determining instrument 
    channel operability and do not change the system function, or 
    channel operation or calibration. Operation within the AV ensures 
    the instrument channel's ability to provide the required reactor 
    trip or engineered safety feature actuation signal during plant 
    operation. In all cases, the proposed changes only make the twelve 
    AVs more restrictive with respect to the current AVs, and do not 
    effect the response characteristics of the instrumentation because 
    actual trip setpoints are unchanged. There is no change being made 
    to the approved design, nor is there any operational change being 
    made which would increase the probability of occurrence of an 
    accident previously evaluated. The RTS [Reactor Trip System] and 
    ESFAS [Engineered Safety Feature Actuation System] systems which are 
    actuated by the corresponding instrumentation setpoints will operate 
    in the same manner as before and within their design limits.
        These changes to the twelve AVs do not involve an increase in 
    the consequences of an accident previously evaluated. These changes 
    have no effect on plant operation. There is no physical or 
    operational change being made which would alter the sequence of 
    events, plant response, or assumptions or conclusions of the 
    affected analyses. The use of the AVs as a basis for determining 
    instrument or channel operability does not change system operation 
    or channel function. The proposed changes do not change the 
    established trip setpoints for these functions. No design analyses 
    have changed or will be affected. The twelve revised AVs are more 
    restrictive than the current AVs and continue to ensure that the 
    safety limits are not violated during anticipated transients, and 
    that the consequences of design basis accidents remain acceptable. 
    The change to the AVs does not degrade or prevent any actions from 
    taking place in response to an accident. The use of NRC approved or 
    endorsed methodology in developing the proposed AVs ensures that the 
    present analytical limits for all accidents will be maintained. 
    These proposed changes to the AVs for RTS and ESFAS instrumentation 
    will continue to ensure that the associated RTS trip or ESFAS 
    actuation signals will be generated when required within the bounds 
    of the plant safety analyses. There is no change in the type or 
    amount of any effluents released, and no change in either the onsite 
    or offsite dose consequences as a result of this change.
        Therefore, based on this evaluation, this proposed amendment 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        These proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The proposed changes to the twelve AVs for RTS and ESFAS 
    instrumentation will not affect the trip setpoints at which a 
    reactor trip or engineered safety feature actuation is initiated. 
    The trip setpoints contained in the Technical Requirements Manual 
    are not being changed and will continue to be maintained. The only 
    changes being made are to the AVs used as a basis for determining 
    instrument channel operability. Because the trip setpoints are 
    unchanged, RTS or ESFAS setpoint actuation is not affected by the 
    revised AVs.
        An RTS trip or ESFAS actuation signal that may initiate between 
    its trip setpoint and the associated AV is acceptable because an 
    allowance has been made in the affected instrument uncertainty 
    calculation to accommodate this deviation. It allows for potential 
    drift while ensuring plant operation in a safe manner. Using this 
    methodology provides plant operational flexibility and yet remains 
    within the allowances accounted for in the various accident 
    analyses. No new equipment is being installed, and no installed 
    equipment is being operated in a new or different manner with these 
    twelve AV changes. The revised AVs do not alter the intended design 
    or operation of systems or instrument channels.
        As no physical plant equipment changes are being made, no new 
    equipment failure modes are being introduced as a result of these 
    proposed changes. There is no change in plant operation that affects 
    previously evaluated failure modes and no change in plant response 
    to a transient condition. These changes do not represent a new 
    failure mode over what has been previously evaluated.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        There is no significant reduction in the margin of safety from 
    these proposed changes. These proposed changes move twelve AVs 
    closer to the trip setpoints compared to the existing AVs, which 
    increases the margin of safety. An RTS trip or ESFAS actuation 
    signal that may initiate between its trip setpoint and the 
    associated AV is acceptable because an allowance has been made in 
    the affected instrument uncertainty calculation to accommodate this 
    deviation. The revised AVs have been calculated using NRC approved 
    or endorsed methodology, which is consistent with existing safety 
    analyses that define the margin of safety. Safety analyses 
    assumptions and results are not affected.
        Therefore, these changes do not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Ms. Pamela B. Stroebel, Senior Vice 
    President and General Counsel, Commonwealth Edison Company, P.O. Box 
    767, Chicago, Illinois 60690-0767.
        NRC Project Director: Stuart A. Richards.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of amendment request: January 21, 1999.
        Description of amendment request: This amendment request proposes 
    to relocate Technical Specification (TS) Section 3/4.6.I to the Updated 
    Final Safety Analysis Report (UFSAR) and plant procedures. TS Section 
    3/4.6.I contains reactor coolant chemistry limiting conditions for 
    operation (LCO) and surveillance requirements (SR) for conductivity, 
    chloride concentration and pH.
    
    [[Page 9187]]
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes simplify the TS, meet regulatory 
    requirements for relocated TS's, and implement the recommendations 
    of the Commission's Final Policy Statement on TS improvements. The 
    Chemistry requirements will be relocated to the Updated Final Safety 
    Analysis Report (UFSAR) and to applicable station procedures. Future 
    changes to these requirements will be controlled by 10 CFR 50.59. 
    The proposed changes are administrative in nature and do not involve 
    any modification to any plant equipment or affect plant operation. 
    Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of any previously 
    evaluated accident.
        Consequently, this proposed amendment does not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated.
        Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes are administrative in nature, do not 
    involve any physical alterations to any plant equipment, and cause 
    no change in the method by which any safety related system performs 
    its function. Therefore, this proposed TS amendment will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        Does the change involve a significant reduction in a margin of 
    safety?
        The proposed amendment represents the relocation of current 
    requirements which are based on generic guidance or previously 
    approved provisions for other stations. The proposed changes are 
    administrative in nature and do not adversely affect existing plant 
    safety margins or the reliability of the equipment assumed to 
    operate in the safety analysis. The proposed changes have been 
    evaluated and found to be acceptable for use at Quad Cities Nuclear 
    Power Station. Since the proposed changes are administrative in 
    nature, and are based on NRC accepted provisions which have been 
    adopted at other nuclear facilities, and maintain the necessary 
    levels of system reliability, the proposed changes do not involve a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
        Attorney for licensee: Ms. Pamela B. Stroebel, Senior Vice 
    President and General Counsel, Commonwealth Edison Company, P.O. Box 
    767, Chicago, Illinois 60690-0767.
        NRC Project Director: Stuart A. Richards.
    
    Duke Energy Corporation (DEC), et al., Docket Nos. 50-413 and 50-414, 
    Catawba Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: January 28, 1999.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications (TS) to correct Surveillance 
    Requirement (SR) 3.7.13.4 and the associated Bases. This SR currently 
    is incorrect and does not reflect the Fuel Handling Ventilation Exhaust 
    System (FHVES) as designed. Specifically, the FHVES flow rate 
    requirement has been inadvertently stated at half the design value 
    (18,221 instead of 36,443 cfm [cubic feet per minute]). The proposed 
    amendments would only revise the SR to the correct design value; no 
    physical change to the FHVES design is involved.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    First Standard
    
        Implementation of this amendment would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. Approval of this amendment will have no effect 
    on accident probabilities or consequences. The FHVES is not an 
    accident initiating system; therefore, there will be no impact on 
    any accident probabilities by the approval of this amendment. The 
    design of the system is not being modified by this proposed 
    amendment. The amendment merely aligns TS requirements with the 
    existing design and function of the system. Therefore, there will be 
    no impact on any accident consequences.
    
    Second Standard
    
        Implementation of this amendment would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. No new accident causal mechanisms are created 
    as a result of NRC approval of this amendment request. No changes 
    are being made to the plant which will introduce any new accident 
    causal mechanisms. This amendment request does not impact any plant 
    systems that are accident initiators; neither does it impact any 
    accident mitigating systems.
    
    Third Standard
    
        Implementation of this amendment would not involve a significant 
    reduction in a margin of safety. Margin of safety is related to the 
    confidence in the ability of the fission product barriers to perform 
    their design functions during and following an accident situation. 
    These barriers include the fuel cladding, the reactor coolant 
    system, and the containment system. The performance of these fission 
    product barriers will not be impacted by implementation of this 
    proposed amendment. The FHVES is already capable of performing as 
    designed. No safety margins will be impacted.
        Based upon the preceding analysis, Duke Energy has concluded 
    that the proposed amendment does not involve a significant hazards 
    consideration.
    
        The staff reviewed the licensee's analysis, and agrees that the 
    three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC 
    staff proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
        Attorney for licensee: Mr. Paul R. Newton, Legal Department 
    (PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte, 
    North Carolina.
        NRC Project Director: Herbert N. Berkow.
    
    Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of amendment request: December 16, 1998, supplemented January 
    25, 1999.
        Description of amendment request: The proposed amendments would 
    completely replace the High Pressure Injection (HPI) section of the 
    Improved Technical Specifications that were issued on December 16, 
    1998. The proposed changes would: (1) expand the applicability for the 
    requirements regarding the third HPI pump, discharge crossover valves, 
    and the HPI suction headers; (2) specify the HPI conditions and allowed 
    times that require the discharge headers be cross-connected or 
    separated; (3) incorporate limiting conditions for operation when 
    specified equipment was inoperable during specified plant conditions; 
    (4) specify changes in HPI system discharge path valve lineup when 
    certain equipment is inoperable; (5) change the requirement to reduce 
    reactor power when an HPI system is inoperable from 60 percent power to 
    75 percent power and specify the length of time operation may continue 
    at this power level; (6) address the failure to cross-connect the HPI
    
    [[Page 9188]]
    
    discharge headers as an independent condition; (7) add a requirement to 
    verify by administrative means that the Atmospheric Dump Valve flow 
    path for each steam generator is operable every 12 hours under certain 
    conditions; (8) add a requirement that the HPI pump and crossover 
    valves be restored to operable status within 30 days; (9) delete the 
    requirement to restore the capability to automatically actuate the HPI 
    within 24 hours; (10) add a Required Action to reduce reactor power to 
    less than or equal to 75 percent power within 3 hours in the event an 
    HPI train cannot be actuated by automatic or manual means; (11) expand 
    the Completion Time for restoring an inoperable HPI train to 72 hours; 
    (12) require that Limiting Condition for Operation 3.0.3 be entered 
    immediately if two HPI trains or two HPI (low pressure injection) -LPI 
    flow paths are inoperable; (13) change the surveillance requirement to 
    manually cycle open each LPI-HPI flow path discharge valve every 18 
    months to require that the HPI discharge crossover valves be cycled 
    every 18 months; and (14) add or modify various administrative and 
    Bases changes that support the proposed changes. The licensee supplied 
    data resulting from risk-informed analyses that were performed in 
    accordance with Regulatory Guides 1.174 and 1.177 to support the 
    evaluation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated:
        No. The proposed change do not involve a physical alteration of 
    the plant. No new or different equipment is being installed, and no 
    installed equipment is being operated in a new or different manner. 
    No set points for parameters which initiate protective or mitigative 
    action are being changed.
        The proposed changes do not have any impact upon the ability of 
    the HPI [High Pressure Injection] System to add soluble poison to 
    the Reactor Coolant System. The remaining potential impact is upon 
    the ability to mitigate the consequences of a small break LOCA 
    [Loss-of-Coolant Accident], which is addressed below. The small 
    break LOCA is the limiting design basis accident with respect to HPI 
    System operability requirements.
        The Technical Specification requirements for the HPI System are 
    supported by a spectrum of small break LOCA analyses based on the 
    approved Evaluation Model described in FTI [Framatome Technologies 
    Incorporated] topical report BAW-10192PA. These small break LOCA 
    analyses demonstrate that the acceptance criteria of 10 CFR 50.46 
    are satisfied.
        The requirements of LCO [Limiting Condition for Operation] 3.5.2 
    assure that flow can be provided via two HPI trains (i.e., one HPI 
    train responds automatically upon an ESPS [Engineered Safeguards 
    Protective System] signal, and the second HPI train is aligned 
    within 10 minutes via operator actions in the Control Room) 
    following a small break LOCA and a single active failure. The full 
    power small break LOCA analyses supporting this proposed license 
    amendment have been performed in accordance with the approved 
    Evaluation Model described in FTI topical report BAW-10192P.
        If enhanced steam generator cooling is not credited in the 
    accident analysis, two HPI trains are required to mitigate specific 
    small break LOCAs with Thermal Power [less than or equal to] 75% RTP 
    [Reactor Thermal Power]. However, if equipment not qualified as QA-1 
    (i.e., an ADV [Atmosphic Dump Valve] flow path for one steam 
    generator) is credited for enhanced steam generator cooling, the 
    safety analyses have determined that the capacity of one HPI train 
    is sufficient to mitigate a small break LOCA on the discharge of the 
    reactor coolant pumps if Thermal Power [less than or equal to] 75% 
    RTP. An ADV flow path for each steam generator is credited as a 
    compensatory measure in Actions B and C of LCO 3.5.2 to permit 
    operation to continue with THERMAL POWER [less than or equal to] 75% 
    RTP: a) for 30 days with an HPI pump of one or more HPI discharge 
    crossover valve(s) inoperable; and b) for 72 hours with one HPI 
    train inoperable. This provides additional defense-in-depth, because 
    the ADV flow path for each steam generator is required to be 
    operable while only one is needed to perform the function. 
    Additionally, a risk-informed assessment (provided as Attachment 7 
    to Duke's license amendment request dated December 18, 1998) 
    concluded that operating the plant in accordance with the Required 
    Actions was acceptable.
        The proposed changes involve crediting an additional operator 
    action (i.e., steaming that steam generator through an ADV flow 
    path) that has not previously been reviewed and approved by the 
    staff for licensing basis small break LOCA analyses. Additionally, 
    while the EFW System has been credited in past SBLOCA [small break 
    LOCA] analyses as described in responses to NUREG-0565, actions to 
    raise steam generator levels to the loss of subcooled margin 
    setpoint were only assumed in the smaller SBLOCAs. These operator 
    actions have been included in the Emergency Operating Procedure 
    (i.e., AP/1, 2, or 3/A/1800/001) for many years.
        The times for completing these operator actions (i.e., feeding a 
    steam generator via EFW [Emergency Feedwater] and steaming that 
    steam generator through an ADV flow path) are new to the small break 
    LOCA analysis and the licensing basis, and are considered 
    reasonable. Crediting the performance of these operator actions 
    within the specified time frames in the SBLOCA analyses does not 
    result in any substantive change to the operator's response to [an] 
    SBLOCA.
        In summary, the technical analyses described in this license 
    amendment justify the adequacy of this specification and assure that 
    operability of the HPI System is maintained in a manner consistent 
    with the requirements of the design basis accidents. Therefore, it 
    is concluded that this amendment request will not significantly 
    increase the probability or consequences of an accident previously 
    evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any kind of accident previously evaluated:
        No. The proposed changes do not involve a physical alteration of 
    the plant. No new or different equipment is being installed, and no 
    installed equipment is being operated in a new or different manner. 
    No set points for parameters which initiate protective or mitigative 
    action are being changed. As a result, no new failure modes are 
    being introduced.
        The requirements of ITS [Improved Technical Specification] 3.5.2 
    continue to assure that operability of the HPI System is maintained 
    in a manner consistent with the requirements of the design basis 
    accidents. The requirements are supported by small break LOCA 
    analyses which demonstrate that the acceptance criteria of 10 CFR 
    50.46 are satisfied.
        The proposed change involve crediting an additional operator 
    action (i.e., steaming that steam generator through an ADV flow 
    path) that has not previously been reviewed and approved by the 
    staff for licensing basis small break LOCA analyses. Additionally, 
    while the EFW System has been credited in past SBLOCA analyses as 
    described in responses to NUREG-0565, actions to raise steam 
    generator levels to the loss of subcooled margin setpoint were only 
    assumed in the smaller SBLOCAs. These operator actions have been 
    included in the Emergency Operating Procedure (i.e., AP/1, 2, or 3/
    A/1800/001) for many years.
        The times for completing these operator actions (i.e., feeding a 
    steam generator via EFW and steaming that steam generator through an 
    ADV flow path) are new to the small break LOCA analysis and the 
    licensing basis, and are considered reasonable. Crediting the 
    performance of these operator actions within the specified time 
    frames in the SBLOCA analyses does not result in any substantive 
    change to the operator's response to [an] SBLOCA.
        Therefore, this proposed amendment will not create the 
    possibility of any new or different kind of accident.
        (3) Involve a significant reduction in a margin of safety.
        No. The requirements of ITS 3.5.2 continue to assure that 
    operability of the HPI System is maintained in a manner consistent 
    with the requirements of the design basis accidents. The 
    requirements are supported by small break LOCA analyses which 
    demonstrate that the acceptance criteria of 10 CFR 50.46 are 
    satisfied. These analyses were performed in accordance with the 
    Evaluation Model described in FTI topical report BAW-10192P.
        Therefore, it is concluded that the proposed amendment request 
    will not result in a significant decrease in the margin of safety.
    
    
    [[Page 9189]]
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC.
        NRC Project Director: Herbert N. Berkow.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of amendment request: January 18, 1999
        Description of amendment request: The proposed amendments would: 
    (1) delete license condition 2.C.(3) from the Beaver Valley Power 
    Station, Unit No. 1 (BVPS-1) operating license and delete some 
    references to two-loop operation from BVPS-1 Technical Specifications 
    (TSs); (2) revise BVPS-1 and Beaver Valley Power Station, Unit No. 2 
    (BVPS-2) TS 2.2.1, 3.3.2.1, associated tables 2.2-1 and 3.3.4, and 
    associated bases, to use consistent format and wording between units; 
    (3) revise BVPS-1 and BVPS-2 TS 2.2.1, 3.3.2.1, associated tables 2.2-1 
    and 3.3.4, and associated bases, to include revised nominal trip 
    setpoints and allowable values which are more conservative than those 
    currently listed; (4) delete or revise TS to reflect the current 
    configuration of Unit 1 plant hardware; and (5) make miscellaneous 
    editorial changes to BVPS-1 and BVPS-2 TS and associated Bases to 
    define terms, revise formatting, modify titles, and add license numbers 
    to pages.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below [as modified by the NRC staff 
    based upon information provided elsewhere in the licensee's submittal].
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        This proposed amendment includes changes to nominal Reactor Trip 
    System (RTS) and Engineered Safety Feature Actuation System (ESFAS) 
    trip setpoints and allowable values that have been determined with 
    the use of an approved methodology. The new values ensure that all 
    automatic protective actions will be initiated at or before the 
    condition assumed in the safety analysis. This change, which 
    includes modification of the requirements stated in Limiting Safety 
    System Setting (LSSS) 2.2.1 and Limiting Condition for Operation 
    (LCO) 3.3.2.1, will allow the nominal trip setpoints to be adjusted 
    within the calibration tolerance band allowed by the setpoint 
    methodology. There will be no adverse effect on the ability of the 
    channels to perform their safety functions as assumed in the safety 
    analyses. Since there will be no adverse effect on the trip 
    setpoints or the instrumentation associated with the trip setpoints, 
    there will be no significant increase in the probability of any 
    accident previously evaluated.
        Other changes in trip system function, content and format are 
    proposed based on the current configuration of the trip system 
    hardware at Beaver Valley Power Station (BVPS) Unit No. 1. 
    Similarly, since the ability of the instrumentation to perform its 
    safety function is not adversely affected, there will be no 
    significant increase in the consequences of any accident previously 
    evaluated.
        Since the safety analysis is unaffected by this change there is 
    no change in the consequences of any previously evaluated accident.
        The editorial changes do not affect plant safety. The 
    administrative change, for BVPS Unit 1 only, pertaining to two loop 
    operation and Reactor Coolant System isolation valve position, does 
    not affect plant safety. The Technical Specification requirements in 
    LCOs 3.4.1.1 and 3.4.1.4.1 will continue to [prohibit two-loop 
    operation and] ensure safe plant operation by properly controlling 
    the operation and position of the reactor coolant loops and Reactor 
    Coolant System isolation valves.
    
    [The administrative change to delete line item 7.d, pertaining to 
    Auxiliary Feedwater (AFW) Pump Auto-start on Emergency Bus 
    Undervoltage, from BVPS-1 TS Tables 3.3-3, 3.3-4, and 4.3-2 will not 
    affect plant safety because this function is not directly initiated 
    by bus undervoltage. Rather, the automatic start of the motor-driven 
    AFW pumps is accomplished by the combination of 1) Emergency Bus 
    feed breaker opening 2) valid start signal from ESFAS, and 3) 
    Emergency Diesel Generator (EDG) sequencer actuation. Requirements 
    for these items are included in the ESFAS related TS, Table 3.3-3 
    and 3.3-4 items 7.a, 7.c, 7.e, and EDG related TS 4.8.1.1.2.b.3 (b). 
    Therefore, since there is no change made to the plant hardware or 
    its operation and requirements related to the AFW pump auto-start 
    function are maintained elsewhere in the BVPS-1 TS, deleting line 
    item 7.d from BVPS-1 TS Tables 3.3-3, 3.3-4, and 4.3-2 will not 
    change the probability or consequences of any accident previously 
    evaluated.]
        Therefore, this change does not involve any significant increase 
    in the probability of occurrence of any accident previously 
    evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed amendment includes changes to the format and 
    magnitudes of nominal trip setpoints and allowable values that 
    preserve all safety analysis assumptions related to accident 
    mitigation. The protection system will continue to initiate the 
    protective actions as assumed in the safety analysis. The proposed 
    changes to LSSS 2.2.1 and LCO 3.3.2.1 will continue to ensure that 
    the trip setpoints are maintained consistent with the setpoint 
    methodology and the plant safety analysis. This proposed amendment 
    does not involve additional hardware changes. Plant operation will 
    not be changed.
        Other proposed changes are made so that the Technical 
    Specifications more accurately reflect the plant-specific trip 
    system hardware in BVPS Unit No. 1.
        Furthermore, the proposed changes do not alter the functioning 
    of the RTS and ESFAS. Therefore, the proposed change does not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes do not alter the manner in which safety 
    limits, limiting safety system settings or limiting conditions for 
    operation are determined. The proposed RTS and ESFAS trip setpoints 
    are calculated with an approved methodology. The proposed changes to 
    LSSS 2.2.1 and LCO 3.3.2.1 will continue to ensure that the trip 
    setpoints are maintained consistent with the setpoint methodology 
    and the plant safety analysis. Therefore, the response of the RTS 
    and ESFAS to accident transients reported in the Updated Final 
    Safety Analysis Report is unaffected by this change. No additional 
    hardware changes are involved. Therefore, accident analysis 
    acceptance criteria are not affected. Other proposed changes are 
    made so that the protection system Technical Specifications more 
    accurately reflect the plant-specific trip system hardware in BVPS 
    Unit No. 1.
        The editorial changes do not affect plant safety. The 
    administrative change, for BVPS Unit 1 only, pertaining to two loop 
    operation and Reactor Coolant System isolation valve position, does 
    not affect plant safety. The Technical Specification requirements in 
    LCOs 3.4.1.1 and 3.4.1.4.1 will continue to [prohibit two-loop 
    operation and] ensure safe plant operation by properly controlling 
    the operation and position of the reactor coolant loops and Reactor 
    Coolant System isolation valve.
    
    [The administrative change to delete line item 7.d, pertaining to 
    Auxiliary Feedwater (AFW) Pump Auto-start on Emergency Bus 
    Undervoltage, from BVPS-1 TS Tables 3.3-3, 3.3-4, and 4.3-2 will not 
    affect plant safety because this function is not directly initiated 
    by bus undervoltage. Rather, the automatic start of the motor-driven 
    AFW pumps is accomplished by the combination of (1) Emergency Bus 
    feed breaker opening, (2) valid start signal from ESFAS, and (3) EDG 
    sequencer actuation. Requirements for these items are included in 
    the ESFAS related TS, Table 3.3-3 and 3.3-4 items 7.a, 7.c, 7.e, and 
    EDG related TS 4.8.1.1.2.b.3 (b). Therefore, since there is no 
    change made to the plant hardware or its operation and requirements 
    related to the AFW pump auto-start function are maintained elsewhere 
    in the BVPS-1 TS,
    
    [[Page 9190]]
    
    deleting line item 7.d from BVPS-1 TS Tables 3.3-3, 3.3-4, and 4.3-2 
    will not involve a significant reduction in a margin of safety.]
        Therefore, operation of the facility in accordance with the 
    proposed amendment will not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B.F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: S. Singh Bajwa.
    
    Entergy Gulf States, Inc., and Entergy Operations, Inc., Docket No. 50-
    458, River Bend Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: December 16, 1998.
        Description of amendment request: The licensee has proposed an 
    amendment of Facility Operating License No. NPF-47, Appendix A--
    Technical Specifications, Section 2.1.1.2, entitled ``Reactor Core 
    [Safety Limits].'' The proposed amendment will change the two 
    recirculation loop Minimum Critical Power Ratio (MCPR) limit from 1.13 
    to 1.12 and the single recirculation loop MCPR limit from 1.14 to 1.13. 
    The revised limits are necessary to address the operation of Cycle 9 
    following the refueling outage which is scheduled to begin April 1999.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The request does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The plant/cycle specific SLMCPRs have been calculated using 
    methods identical to those used by General Electric (GE) to assess 
    the SLMCPR for other Boiling Water Reactors (BWRs). Similar methods 
    were used to determine the value of the SLMCPR for the previous 
    cycle. These methods are within the existing design and licensing 
    basis and cannot increase the probability or severity of an 
    accident. The basis of the SLMCPR calculation is to ensure that 
    greater than 99.9% of all fuel rods in the core avoid transition 
    boiling and fuel damage in the event of the occurrence of 
    Anticipated Operational Occurrences (AOO) or a postulated accident.
        The SLMCPR is used to establish the Operating Limit Minimum 
    Critical Power Ratio (OLMCPR). Neither the SLMCPR nor the OLMCPR are 
    initiators or affect initiators of an accident previously evaluated 
    and therefore changes to the SLMCPR do not increase the probability 
    of any accident previously evaluated. The proposed changes involve 
    the use of an accepted methodology in calculating the SLMCPR and, 
    since there is no change in the definition of the SLMCPR, these 
    changes will not affect the consequences of any accident previously 
    evaluated. In addition, the proposed changes do not involve any 
    change in the way the plant is operated. Existing procedures will 
    ensure that the SLMCPR is not violated. Therefore, these changes 
    have no effect on the consequences of an accident.
        On these bases, there will be no increase in the probability or 
    consequences of an accident previously analyzed as a result the 
    proposed changes.
        2. The request does not create the possibility of occurrence of 
    a new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes consist of SLMCPR calculated from an 
    accepted method of analysis that has been used by many BWRs. These 
    changes do not involve any alteration of the plant and do not affect 
    the plant operation. Neither the SLMCPR nor the OLMCPR can initiate 
    an event, therefore a change to the SLMCPR does not create the 
    possibility of occurrence of a new or different kind of accident 
    from any accident previously evaluated.
        3. The request does not involve a significant reduction in the 
    margin of safety.
        The SLMCPR is a Technical Specification numerical value to 
    ensure that 99.9% of all fuel rods in the core will avoid transition 
    boiling if the limit is not violated. The proposed SLMCPR change 
    results from SLMCPR analysis using the accepted methods as 
    identified in the Attachment.
        The margin of safety resides between the SLMCPR and the point at 
    which fuel fails. Maintaining the MCPR above the proposed SLMCPR 
    will maintain the margin of safety associated with GE's SLMCPR 
    methodology. Existing plant procedures will continue to ensure that 
    the SLMCPR is not violated.
        Therefore, this request does not involve a reduction in the 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803.
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: December 23, 1998.
        Description of amendment request: The proposed changes will modify 
    the Limiting Condition for Operation for Technical Specifications 
    3.3.3.7.1 for the chlorine detection system at Waterford Steam Electric 
    Station, Unit 3. A change in the alarm/trip setpoint from 3 parts per 
    million (ppm) to 2 ppm is requested. Additionally, the proposed request 
    corrects a typographical error in Table 3.3-4.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: The chlorine detection system has no effect on the 
    accidents analyzed in Chapter 15 of the Final Safety Analysis 
    Report. Its only effect is on habitability of the control room, 
    which will be enhanced by specifying a more conservative setpoint in 
    the Technical Specifications (TS). Analysis using more conservative 
    assumptions show that a setpoint of 2 parts per million (ppm) 
    chlorine is acceptable.
        Correcting the typographical error on TS page 3/4 3-19 has no 
    effect on the probability or consequences of an accident previously 
    evaluated.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: The proposed Technical Specification change in itself 
    does not change the design or configuration of the plant. Using a 
    more conservative setpoint performs the same function as the old 
    setpoint, but it accomplishes this function with increased 
    conservatism.
        Correcting the typographical error on TS page 3/4 3-19 will not 
    create the possibility of a new or different type of accident from 
    any accident previously evaluated.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change
    
    [[Page 9191]]
    
    involve a significant reduction in a margin of safety?
        Response: The chlorine detection system has no effect on a 
    margin of safety as defined by Section 2 of the Technical 
    Specifications. Its only effect is on habitability of the control 
    room, which will be enhanced by a more conservative setpoint 
    provided by this change to the Technical Specifications.
        Correcting the typographical error on TS page 3/4 3-19 does not 
    involve a significant reduction in a margin of safety.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn, 1400 
    L Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: John N. Hannon.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: January 25, 1999.
        Description of amendment request: The proposed change request will 
    modify Technical Specification (TS) 3.5.1 to allow up to 72 hours to 
    restore safety injection tank (SIT) to operable status if one SIT is 
    inoperable due to boron concentration not within the limits or the 
    inability to verify level and pressure. The proposed change would also 
    allow up to 24 hours to restore SIT to operable status if one SIT is 
    inoperable due to other reasons when Reactor Coolant System pressure is 
    greater than or equal to 1750 psia. The ACTIONS for an inoperable SIT 
    are being subdivided based on pressurizer pressure to be consistent 
    with the current Waterford 3 requirements and applicability. 
    Additionally, the Surveillance requirement to sample the SIT after a 1% 
    volume increase is being changed to not be required if the source of 
    the makeup is the refueling water storage pool. This amendment request 
    is a collaborative effort of participating Combustion Engineering 
    Owners Group members based on a review of plant operations, 
    deterministic and design basis considerations, and plant risk, as well 
    as previous generic studies and conclusions drawn by the NRC Staff and 
    contained within NUREG-1366, ``Improvements to Technical Specifications 
    Surveillance Requirements,'' and NUREG-1432, Revision 1, ``Standard 
    Technical Specifications for Combustion Engineering (CE) Plants.'' TS 
    Bases 3/4.5.1 will be revised to support above changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: The Safety Injection Tanks (SITs) are passive 
    components in the Emergency Core Cooling System. The SITs are not an 
    accident initiator in any accident previously evaluated. Therefore, 
    this change does not involve an increase in the probability of an 
    accident previously evaluated.
        The SITs were designed to mitigate the consequences of Loss of 
    Coolant Accidents (LOCA). These proposed changes do not affect any 
    of the assumptions used in deterministic LOCA analyses. Hence the 
    consequences of accidents previously evaluated do not change.
        In order to fully evaluate the affect of the SIT Allowed Outage 
    Time (AOT) extension from 1 hour to 24 hours when one SIT is 
    inoperable for reasons other than boron concentration or inability 
    to measure level or pressure, probabilistic safety analysis (PSA) 
    methods were utilized. The results of these analyses show no 
    significant increase in the core damage frequency. As a result, 
    there would be no significant increase in the consequences of an 
    accident previously evaluated. These analyses are detailed in CE 
    NPSD-994, Combustion Engineering Owners Group ``Joint Applications 
    Report for Safety Injection Tank AOT/STI Extension.''
        The proposed change to extend the AOT from 1 hour to 72 hours 
    when unable to measure level or pressure is acceptable because SIT 
    operability is not based on instrumentation availability. Therefore, 
    this does not involve a significant increase in the consequences of 
    an accident as evaluated and are endorsed by the Nuclear Regulatory 
    Commission (NRC) in NUREG-1366, ``Improvements to Technical 
    Specifications Surveillance Requirements.'' The inability to measure 
    level or pressure is acceptable because the SIT instrumentation 
    provides no safety actuation.
        The AOT extension from 1 hour to 72 hours, based upon boron 
    concentration outside the prescribed limits does not involve a 
    significant increase in the consequences of an accident as evaluated 
    and approved by the NRC in NUREG-1432, ``Standard Technical 
    Specifications for Combustion Engineering Plants.'' These changes 
    are acceptable because the reduced concentration effects on core 
    subcriticality during reflood are minor.
        The change in sampling requirements to not require sampling if 
    the makeup source is of the same concentration limit as the SIT is 
    acceptable as the concentration will remain within the TS limits.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different kind of 
    accident from any accident previously evaluated?
        Response: The proposed change does not alter the design or 
    configuration of the plant. It also does not alter the mitigation 
    capabilities of any safety system or components. This change 
    increases the AOTs for the condition of SIT inoperability. The boron 
    concentration is maintained by make-up from a source of water with 
    the required concentration of the SITs.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: The proposed changes do not affect the limiting 
    conditions for operation or their bases that are used in the 
    deterministic analyses to establish the margin of safety. PSA and 
    deterministic evaluations were used to evaluate these changes. The 
    PSA evaluations demonstrated that the applicable changes are either 
    risk neutral or risk beneficial. These evaluations are detailed in 
    CE NPSD-994. The deterministic evaluations show that the SITs would 
    be able to perform their safety function. These changes are 
    consistent with NUREG-1366 and NUREG-1432. The margin of safety is 
    not significantly affected by makeup from a source of the same 
    concentration limit as the SIT or increase in the AOT for boron 
    concentration of one SIT not within limits.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn, 1400 
    L Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: John N. Hannon.
    
    [[Page 9192]]
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: January 25, 1999.
        Description of amendment request: The proposed changes modify 
    Technical Specifications Section 6.0 to remove certain administrative 
    controls and instead rely on the change controls of 10 CFR 50.54(a)(3) 
    and to add a requirement to Section 6.0 concerning the responsibilities 
    of the General Manager Plant Operations. The requested changes are 
    consistent with the Improved Standard Technical Specifications for 
    Combustion Engineering plants, NUREG-1432.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: The requested changes are purely administrative in 
    nature. The proposed changes do not affect the operation of any 
    structures, systems, or components or the assumptions of any 
    accident analyses. The requested changes only affect Section 6.0 of 
    the Waterford 3 Technical Specifications which describe the 
    administrative controls to be implemented at the site. The requested 
    changes either add an additional administrative requirement or 
    remove quality assurance program details from the Technical 
    Specifications. The details are being removed from the Technical 
    Specifications and instead rely on the change controls of 10 CFR 
    50.54(a)(3). This submittal makes no changes to the regulatory 
    controls governing changes. The requested changes are purely 
    administrative in nature.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different kind of 
    accident from any accident previously evaluated?
        Response: The proposed changes to the Technical Specification 
    requirements are purely administrative in nature and do not involve 
    a change in plant design or affect the configuration or operation of 
    any structure, system, or component.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: The proposed changes do not affect the operation of 
    any structures, systems, or components or the assumptions of any 
    accident analyses. The requested changes are purely administrative 
    in nature.
    
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety. The NRC staff has reviewed the 
    licensee's analysis and, based on this review, it appears that the 
    three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC 
    staff proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn, 1400 
    L Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: John N. Hannon.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of amendment request: January 22, 1999.
        Description of amendment request: The proposed amendment would 
    revise Duane Arnold Energy Center (DAEC) Technical Specification (TS) 
    Section 4.3, ``Fuel Storage,'' by updating the criticality requirements 
    (k-infinity and U-235 enrichment limits) for storage of fuel assemblies 
    in the spent fuel racks. This change would allow for storage of nuclear 
    fuel assemblies with new designs, including GE-12 with a 10X10 pin 
    array.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        After reviewing this proposed amendment, we have concluded:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The probability of occurrence of the accident/abnormal 
    conditions evaluated in UFSAR Section 9.1.2.3 is not significantly 
    increased by this change because no modification in fuel handling 
    equipment, fuel pool cooling equipment, fuel storage racks, or fuel 
    handling practices is taking place. Only the k-infinity and 
    enrichment limits for the stored fuel are being changed.
        The postulated accident/abnormal conditions evaluated in UFSAR 
    Section 9.1.2.3 have been re-evaluated for the proposed changes in 
    k-infinity and enrichment limits. The results demonstrate that the 
    consequences are negligible. The analyses performed show that the 
    requirement to maintain K-eff less than 0.95 (substantially 
    subcritical) is satisfied for normal and postulated abnormal 
    conditions using methods and assumptions that are consistent with 
    the existing UFSAR. Seismic adequacy and structural integrity of the 
    pool and racks are not affected by the introduction of GE-12 fuel. 
    Local and bulk pool temperatures remain bounded by the current UFSAR 
    analysis for fuel exposures with GE-12 fuel expected through two 
    cycles of operation (i.e., through Cycle 18 operation). Based upon a 
    scoping study comparing the hydraulic diameters of GE-10 and GE-12 
    fuel, large margins to pool boiling conditions at the final 
    discharge exposures of GE-12 fuel will be maintained. Therefore, the 
    consequences of the accident are not significantly increased by this 
    change.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        No new types of accidents are being introduced because no 
    modification in fuel handling equipment, fuel pool cooling 
    equipment, fuel storage racks or fuel handling procedures is being 
    made. The design basis function of the spent fuel racks is to 
    maintain the fuel configuration substantially subcritical and within 
    allowable temperatures under both normal and postulated abnormal 
    conditions. This design basis function will be maintained with the 
    proposed k-infinity and enrichment limits.
        3. The proposed amendment will not involve a significant 
    reduction in a margin of safety.
        The margin of safety is not significantly reduced. This margin 
    is based on the requirement to limit the K-eff of fuel in the spent 
    fuel racks to less than 0.95. The proposed changes in k-infinity and 
    enrichment limits have been shown to meet this requirement, using 
    methods and assumptions that are consistent with the existing UFSAR. 
    Seismic adequacy and structural integrity of the pool and racks are 
    not affected by the introduction of GE-12 fuel. Local and bulk pool 
    temperatures remain bounded by the current UFSAR analysis for fuel 
    exposures with GE-12 fuel expected through two cycles of operation 
    (i.e., through Cycle 18 operation). Based upon a scoping study 
    comparing the hydraulic diameters of GE-10 and GE-12 fuel, large 
    margins to pool boiling conditions at the final discharge exposures 
    of GE-12 fuel will be maintained.
        Based upon the above, we have determined that the proposed 
    amendment will not involve a significant hazards consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, IA 52401.
    
    [[Page 9193]]
    
        Attorney for licensee: Jack Newman, Al Gutterman, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: Cynthia A. Carpenter.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of amendment request: October 15, 1998, as supplemented on 
    December 21, 1998.
        Description of amendment request: The proposed amendment would 
    revise the Duane Arnold Energy Center (DAEC) Technical Specifications 
    (TS) by adding a new TS 3.7.9, ``Control Building/Standby Gas Treatment 
    System (CB/SBGT) Instrument Air System.'' The proposed amendment would 
    also revise (TS) 3.6.1.3, ``Primary Containment Isolation Valves 
    (PCIVs),'' Condition E, by adding a time limit for plant operation if a 
    penetration flow path is isolated by a single purge valve with 
    resilient seal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The amendment is adding new requirements for the CB/SBGT 
    Instrument Air System that are commensurate with the safety 
    functions it supports and consistent with other support systems in 
    the Technical Specifications. These requirements provide appropriate 
    actions and time limits for plant operation with one or both CB/SBGT 
    Instrument Air subsystems inoperable. The probability of an event 
    while in this condition is low, and the consequences are bounded by 
    the failure of the supported systems. The CB/SBGT Instrument Air 
    System is not assumed to be an initiator of an analyzed event.
        The amendment is also adding a time limit for plant operation if 
    a purge valve with resilient seal is used to satisfy TS 3.6.1.3 
    Required Action E.1 (isolate the affected penetration flow path). 
    While primary containment integrity is provided by the purge valve, 
    it is prudent to limit operation in this condition due to the 
    potential for increased leakage from a single active failure.
        These additions will provide assurance that affected systems 
    will be OPERABLE when required and as assumed in the design basis.
        This change will not physically alter the plant (no new or 
    different type of equipment will be installed). This change will not 
    alter the operation of process variables, structures, systems, or 
    components as described in the safety analysis. This change will not 
    alter assumptions relative to the mitigation of an accident or 
    transient event. This change will not increase the probability of 
    initiating, or the consequences of an analyzed event.
        (2) The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The amendment adds new requirements for the CB/SBGT Instrument 
    Air System and adds a time limit for plant operation if a purge 
    valve with resilient seal is used to satisfy TS 3.6.1.3 Required 
    Action E.1.
        This change will not physically alter the plant (no new or 
    different type of equipment will be installed). This change will not 
    alter the operation of process variables, structures, systems, or 
    components as described in the safety analysis. Thus, a new or 
    different kind of accident will not be created.
        (3) The proposed amendment will not involve a significant 
    reduction in a margin of safety.
        The amendment is adding new requirements for the CB/SBGT 
    Instrument Air System to provide appropriate actions and time limits 
    for plant operation with one or both CB/SBGT Instrument Air 
    subsystems inoperable.
        The amendment is also adding a time limit for plant operation if 
    a purge valve with resilient seal is used to satisfy TS 3.6.1.3 
    Required Action E.1 (isolate the affected penetration flow path). 
    While primary containment integrity is provided by the purge valve, 
    it is prudent to limit operation in this condition due to the 
    potential for increased leakage from a single active failure in the 
    remaining OPERABLE components.
        This change will not physically alter the plant (no new or 
    different type of equipment will be installed). This change will not 
    alter the operation of process variables, structures, systems, or 
    components as described in the safety analysis. This change will not 
    alter assumptions relative to the primary success path for 
    mitigation of an accident or transient event.
        These additions will provide assurance that the accident 
    mitigation functions will perform as assumed in the safety analysis. 
    Thus, the margin of safety will not be reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, IA 52401.
        Attorney for licensee: Jack Newman, Al Gutterman, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: Cynthia A. Carpenter.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: January 29, 1999.
        Description of amendment request: The amendment would revise the 
    technical specifications (TS) to relocate three cycle-specific 
    parameter limits; shutdown margin with Tcold>210 deg.F, 
    moderator temperature coefficient, and minimum boric acid storage tank 
    level versus concentration, to the Core Operating Limits Report (COLR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The safety analysis most impacted by a change to the negative 
    Moderator Temperature Coefficient (MTC) limit is the Main Steam Line 
    Break (MSLB) event. The Steam Line Break Cooldown curves for an MTC 
    are calculated and then input to the cycle-specific MSLB analysis 
    (if necessary) during the reload analysis process, using an NRC-
    approved methodology. The required/acceptable Shutdown Margin (SDM) 
    is dependent upon the core loading pattern used (i.e., cycle-
    specific core physics parameters) and is largely dependent on the 
    cycle-specific MTC and available scram worth. The SDM is determined 
    based on the analysis of the Hot Zero Power (HZP) MSLB event in 
    which the return-to-critical and return-to-power conditions are 
    evaluated to provide acceptable results. With the ongoing changes in 
    MTC as a result of core loadings for FCS and higher U-235 
    enrichments, the end-of-cycle MTC is becoming more negative than the 
    present Technical Specifications limit. Since the MTC is fuel cycle 
    specific and influences the required SDM, it is appropriate to move 
    both of these values to the COLR, consistent with Generic Letter 88-
    16. Note that no change to the SDM for Tcold 
    210 deg.F is being proposed.
        The cycle-specific reload analysis is performed for every 
    operating cycle and the results, as incorporated into the COLR 
    pursuant to the 10 CFR 50.59 process, are transmitted to the NRC. 
    FCS will continue to provide COLR updates to the NRC. The relocation 
    of the negative MTC and the ``BAST level versus BAST Concentration'' 
    curves into the COLR, consistent with the NRC recommendations of 
    Generic Letter 88-16, will not modify the methodology used in 
    generating the limits, nor the manner in which they are implemented. 
    These limits will continue to be determined by analyzing the same 
    postulated events as previously analyzed. FCS will continue to 
    operate within the limits specified in the COLR and will take the 
    same corrective actions when or if these limits are exceeded as 
    required by
    
    [[Page 9194]]
    
    current Technical Specifications. The potential increase of the 
    absolute magnitude of the negative MTC with Shutdown Margin decrease 
    is evaluated during the COLR reload analysis process in accordance 
    with OPPD's NRC-approved topical report. Therefore, this proposed 
    amendment is administrative in nature and has been concluded not to 
    increase the probability or consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to FCS Technical Specifications were the 
    result of a recommendation from a Generic Letter. Future changes to 
    the parameters being relocated to the COLR can only be performed 
    with approved Reload Analyses. No new or different kind of accident 
    is created by this administrative change because the actual 
    operation of FCS remains unchanged. Therefore the possibility of an 
    accident or malfunction of a different type than previously 
    evaluated in the safety analysis report would not be created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        As indicated above, the implementation of this proposed COLR 
    change, consistent with the guidance of Generic Letter 88-16, makes 
    use of the existing safety analysis methodologies and the resulting 
    limits and setpoints for plant operation. Additionally, the safety 
    analysis acceptance criteria for operation with this proposed 
    amendment have not changed from the criteria used in the current 
    reload analysis. Therefore, the margin of safety as defined in the 
    bases of Technical Specifications is not reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    PECO Energy Company, Docket Nos. 50-352 and 50-353, Limerick Generating 
    Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of amendment request: January 12, 1999.
        Description of amendment request: The proposed change involves 
    revising Technical Specification (TS) Section 3/4.4.2, ``Safety/Relief 
    Valves,'' and TS Bases Sections B 3/4.4.2, B 3/4.5.1 and B 3/4.5.2, to 
    increase the allowable as-found main steam Safety Relief Valve (SRV) 
    code safety function lift setpoint tolerance from plus or minus 1% to 
    plus or minus 3%. This change will also require the as-left SRV code 
    safety function lift setting to be set within plus or minus 1% of the 
    specified nominal lift setpoint prior to reinstallation in the plant. 
    In support of this proposed TS change, the required number of OPERABLE 
    SRVs in Operational Conditions (OPCONs) 1, 2, and 3 will be changed 
    from 11 to 12. The number of SRVs in each lift pressure grouping will 
    remain the same. This proposed TS change does not alter the SRV nominal 
    lift setpoints or the SRV lift setpoint test frequency currently 
    specified by TS Section 3/4.4.2. The proposed change does not change 
    the SRV testing commitment specified in LGS Updated Final Safety 
    Analysis Report (UFSAR) Chapter 5.2.2.10, ``Inspection and Testing.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS changes allow for an increase in the as-found 
    main steam Safety Relief Valve (SRV) setpoint tolerance from plus or 
    minus 1% to plus or minus 3%. The proposed changes also reduce the 
    allowable number of SRVs to be out-of-service from three (3) to two 
    (2). The proposed changes do not alter the SRV nominal lift 
    setpoints or SRV lift setpoint test frequency. The actuation of an 
    SRV is the precursor to the inadvertent opening of a SRV transient, 
    as discussed in Updated Final Safety Analysis Report (UFSAR) Chapter 
    15.1.4. Increasing the allowable as-found SRV code safety function 
    lift setpoint tolerance from plus or minus 1% to plus or minus 3% 
    does have the potential for the minimum SRV simmer margin to be 
    reduced from 113.3 psig to 89.9 psig. A reduction in simmer margin 
    will not directly result in an increase of the probability on an 
    inadvertent self actuation of an SRV. A reduction in simmer margin 
    will reduce the seating force which may initiate leakage. However, 
    this leakage is monitored and corrective actions can be implemented 
    prior to progressing to the point of the potential of an inadvertent 
    actuation. This reduction in SRV simmer margin has been evaluated by 
    the SRV manufacturer and determined to be acceptable; therefore, the 
    probability of an inadvertent SRV actuation remains unchanged. 
    Actuation of an SRV is not a precursor for any other event evaluated 
    in the Safety Analysis Report (SAR).
        The proposed TS changes have been evaluated on both a generic 
    and plant specific basis. The NRC has approved the general approach 
    of this change; however, implementation is contingent on several 
    plant specific evaluations. The required plant specific analyses and 
    evaluations included transient analysis of the anticipated 
    operational transients (AOTs); analysis of the design basis 
    overpressurization event; evaluation of the performance of high 
    pressure systems, motor operated valves, and vessel instrumentation 
    and associated piping; and evaluation of the containment response 
    during Loss-of-Coolant Accident (LOCA) and hydrodynamic loads on the 
    SRV discharge lines and containment. In addition to the plant 
    specific analyses and evaluations required by the NRC, the following 
    items were also considered: ECCS/LOCA [Emergency Core Cooling 
    System] performance, SRV simmer margin, high pressure--low pressure 
    interfaces, i.e., High Energy Line Break (HELB), Station Blackout 
    (SBO), and Fire Safe Shutdown (FSSD), and the short term 
    pressurization phase of an ATWS [anticipated transient without 
    scram] event. These analyses and evaluations show that there is 
    adequate margin to the design core thermal limits and reactor vessel 
    pressure limits using the plus or minus 3% SRV code safety function 
    lift setpoint tolerance and two (2) SRVs out-of-service. The 
    analyses and evaluations also show that the operation of the high 
    pressure injection systems will not be adversely affected, that SRV 
    discharge piping stresses will not be exceeded, and that the 
    containment response during a LOCA will be acceptable.
        Evaluations of the impact of the proposed change on the 
    Equipment Important to Safety have been performed and no adverse 
    conditions were identified. The reactor pressure vessel and attached 
    systems and piping have been evaluated for the impact of this 
    proposed TS change. A plant specific analysis has been performed 
    which indicates that neither the American Society of Mechanical 
    Engineers (ASME) Code upset limits or the TS Safety Limits for the 
    reactor pressure vessel will be exceeded for the limiting event, 
    i.e., Main Steam Isolation Valve (MSIV) closure with flux Scram. The 
    reactor pressure vessel and attached piping design values will not 
    be exceeded. The current high pressure--low pressure interface 
    evaluation utilized nominal SRV setpoints, and therefore, is 
    unaffected. Therefore, the probability of a malfunction of the 
    reactor pressure vessel and attached systems and piping is not 
    increased.
        The nuclear fuel has been evaluated for the impact of the 
    proposed change. Plant specific analyses were performed which 
    indicate that for all abnormal operational transients adequate 
    margin to the limiting thermal limit parameter, i.e., Minimum 
    Critical Power Ratio (MCPR), is maintained. Emergency Core Cooling 
    System (ECCS)/LOCA performance is maintained adequate to meet the 
    requirements of 10CFR50.46. Therefore, the probability of the 
    malfunction of the nuclear fuel is not increased.
        The SRVs have been evaluated for the impact of the proposed TS 
    changes. No physical changes to the SRVs will be made as a result of 
    the proposed TS changes. Adequate simmer margin will be maintained 
    with the increased tolerance to ensure that an inadvertent lifting 
    of a SRV does not occur.
    
    [[Page 9195]]
    
    The increase in SRV discharge flow and reactor vessel pressure due 
    to the potential for higher SRV lift setpoints are bounded by the 
    SRV steam flows and reactor vessel pressure currently used in the 
    evaluation of SRV discharge piping, quencher, quencher support, and 
    hydrodynamic loads on the suppression pool and submerged structures; 
    therefore, the probability of a malfunction of a SRV or associated 
    components and structures is not increased.
        The Containment response during a LOCA has been evaluated for 
    the impact of the proposed change. The major factor in the 
    Containment response to a LOCA is the rate of reactor vessel water 
    inventory loss. The rate of reactor vessel water inventory loss is 
    mainly dependent on reactor decay heat which is not affected by the 
    proposed change. Therefore, the probability of the malfunction of 
    the Containment is not increased.
        The High Pressure Coolant Injection (HPCI) system has been 
    evaluated for the impact of the proposed TS changes. The analysis 
    determined that the HPCI system would not be capable of developing 
    its design flowrate of 5600 gpm at a reactor pressure of 1205 psig 
    (lowest SRV nominal setpoint +3% tolerance) unless the HPCI turbine/
    pump maximum rated speed was increased. However, increasing the HPCI 
    turbine/pump maximum rated speed is prevented due to HPCI pump 
    discharge piping overpressurization concerns. Further analysis has 
    shown that the HPCI system is capable of meeting its required ECCS 
    function design flowrate, and its required non-ECCS flowrate, 
    without any change to the current system operating parameters. 
    Therefore, the probability of a malfunction of the HPCI System is 
    not increased.
        The Reactor Core Isolation Cooling (RCIC) system has been 
    evaluated for the impact of the proposed change. The analysis 
    determined that in order for the RCIC system to be capable of 
    injecting its design flowrate of 600 gpm at a reactor pressure of 
    1205 psig (lowest SRV setpoint of 1170 psig +3% tolerance) the 
    maximum rated speed of the RCIC turbine/pump is required to be 
    increased from 4575 rpm to 4625 rpm. This increase in the RCIC 
    turbine/pump maximum rated speed will reduce the margin to the 
    overspeed trip from 123% to 122.1%. This reduction in the margin to 
    the overspeed trip is acceptable due to the implementation of plant 
    Modification P00210, ``RCIC System Startup Transient Improvement,'' 
    which reduced the amount of turbine/pump speed overshoot during 
    system startup. The RCIC overspeed trip setpoint will not be 
    changed; therefore, a failure of the RCIC turbine/pump (missile 
    hazard or system overpressurization) due to overspeed is not 
    increased. All other RCIC System components will continue to operate 
    within the currently specified design and operating limits. 
    Therefore, the probability of a malfunction of the RCIC System is 
    not increased.
        The Standby Liquid Control (SLC) system has been evaluated for 
    the impact of the proposed change. The SLC system capability of 
    shutting down the reactor during a postulated event in which all or 
    some of the control rods cannot be inserted or during a postulated 
    Anticipated Transient Without Scram (ATWS) event is not impacted by 
    this proposed change. Therefore, the probability of a malfunction of 
    the SLCS is not increased.
        The Control Rod Drive (CRD) system has been evaluated for the 
    impact of the proposed change. The CRD system capability of 
    controlling reactor power during normal plant operation and rapidly 
    inserting control rod blades (Scram) during abnormal plant 
    conditions is not impacted by the proposed change. Therefore, the 
    probability of a malfunction of the CRD system is not increased.
        The Reactor Vessel Instrumentation System has been evaluated for 
    the impact of the proposed change. The Reactor Vessel 
    Instrumentation System will continue to be operated within the 
    current design pressure/temperature requirements; therefore, the 
    probability of a malfunction of the Reactor Vessel Instrumentation 
    System is not increased.
        The LGS, Units 1 and 2, Generic Letter 89-10 Motor-Operated 
    Valve (MOV) Program has been evaluated for the proposed change. The 
    LGS MOV Program currently uses SRV nominal setpoints for 
    differential pressure determinations for valves in which reactor 
    pressure at the SRV setpoint is limiting. Use of nominal SRV 
    setpoints is consistent with current industry practice. Therefore, 
    the probability of a malfunction of a MOV is not increased.
        Reducing the number of SRVs allowed to be out-of-service does 
    not make the consequences of a malfunction of a SRV more severe, 
    since the number of SRVs required to maintain the reactor vessel 
    within ASME Code and TS Safety Limits will be maintained OPERABLE. 
    The proposed change does not result in any changes to the 
    interactions of any system, structure, or component. All systems, 
    structures, and components will continue to function as designed.
        Therefore, the proposed TS changes do not significantly increase 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes allow for an increase in the as-found 
    SRV setpoint tolerance from plus or minus 1% to plus or minus 3%. 
    The proposed TS changes also reduce the allowable number of SRVs to 
    be out-of-service from three (3) to two (2). Generic and plant 
    specific analyses and evaluations indicate that the plant response 
    to any previously evaluated event will remain unchanged. All plant 
    systems, structures, and components will continue to be capable of 
    performing their required safety function as required by event 
    analysis guidance.
        The proposed TS changes do not alter the SRV nominal lift 
    setpoints or SRV lift setpoint test frequency. The operation and 
    response of the affected Equipment Important to Safety is unchanged. 
    All systems, structures, and components will continue to be operated 
    within acceptable operating and/or design parameters. No system, 
    structure, or component will be subjected to a condition that has 
    not been evaluated and determined to be acceptable using the 
    guidance required for specific event analysis.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The proposed TS changes allow for an increase in the as-found 
    SRV setpoint tolerance from plus or minus 1% to plus or minus 3%. 
    The proposed TS changes also reduce the allowable number of SRVs to 
    be out-of-service from three (3) to two (2). The proposed TS changes 
    do not alter the SRV nominal lift setpoints or SRV lift setpoint 
    test frequency. The operation and response of the affected Equipment 
    Important to Safety is unchanged. All systems, structures, and 
    components will continue to be operated within acceptable operating 
    and/or design parameters. While the calculated peak reactor vessel 
    pressure for the ASME overpressure event and the ATWS Pressure 
    Regulator Failure-Open (PREGO) event are higher than those 
    calculated without the increase in setpoint tolerance, both are 
    still within the respective licensing acceptance limits associated 
    with these events. These licensing acceptance limits have been 
    determined by the NRC to provide a sufficient margin of safety.
        The increase in the RCIC system turbine/pump maximum rated speed 
    is within the capability of the system design. The reduction in the 
    margin to the overspeed trip is not a reduction in the margin of 
    safety, since the operation of the RCIC System has demonstrated 
    minimal speed overshoot on system initiation due to the installation 
    of plant Modification P00210, ``RCIC System Startup Transient 
    Improvement.''
        The inability of the HPCI system to be capable of injecting 5600 
    gpm at a reactor pressure of 1205 psig (lowest SRV nominal setpoint 
    of 1170 psig +3% tolerance) is not a reduction in the margin of 
    safety, since analysis for events that would result in high reactor 
    vessel pressure indicate that the HPCI System is capable of 
    providing adequate coolant injection.
        The increase in SRV steam flow and reactor vessel pressure does 
    not reduce the margin of safety associated with the SRVs and 
    associated components and structures since the increased SRV steam 
    flow rate and reactor vessel pressure are bounded by the current 
    design analysis.
        The margin of safety for fuel thermal limits and 10CFR50.46 
    limits is unaffected by the proposed change.
        The margin of safety for the Containment is unaffected by the 
    proposed change.
        The capability of the SLC system to perform its safety function 
    during all required events, using the required guidance for event 
    analysis, is maintained. Therefore, the proposed changes do not 
    reduce the margin of safety provided by the SLC system.
        Therefore, these proposed TS changes do not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this
    
    [[Page 9196]]
    
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101.
        NRC Project Director: William M. Dean.
    
    PECO Energy Company, Docket Nos. 50-352 and 50-353, Limerick Generating 
    Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of amendment request: January 25, 1999.
        Description of amendment request: The proposed Technical 
    Specification (TS) Change Request revises the TS Surveillance 
    Requirement frequencies for Sections 4.8.1.1.2.e.1, 4.8.1.1.2.e.8.a, 
    and 4.8.1.1.2.e.8.b for the Emergency Diesel Generator maintenance 
    inspection outages, the 24-hour endurance run, and for the hot restart 
    test from 18 to 24 months.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The maintenance inspection interval change and the corresponding 
    interval change for the associated 24 hour endurance test and hot 
    restart test which are normally performed in conjunction with the 
    diesel preventive maintenance overhaul inspections, as well as the 
    programmatic improvements addressed here do not involve physical 
    changes that would affect the ability of the EDGs [emergency diesel 
    generators] to perform their safety function. The Emergency Diesel 
    Generator System is not an accident initiator.
        The Surveillance Testing requirements of Technical Specification 
    Section 3/4.8 will continue to verify the operability and 
    reliability of the Emergency Diesel Generator system.
        The proposed changes do not affect the ability of the EDGs to 
    mitigate the consequences of an accident, including the Loss of 
    Coolant Accident (LOCA) coupled with Loss Of Offsite Power accident 
    analyses as presented in Chapter 15 of the LGS [Limerick Generating 
    Station] UFSAR [Updated Final Safety Analysis Report]. EDG 
    unavailability due mostly to outage inspections is more than 2 times 
    higher than EDG unplanned unavailability. An extension of the outage 
    inspection frequency to 24 months will result in increased EDG 
    availability to mitigate the consequences of a potential accident. 
    When this program is taken in its entirety the extended maintenance 
    intervals coupled with the defined enhancements is judged to result 
    in an overall increase in EDG availability and reliability. 
    Therefore, the probability or consequences of an accident previously 
    evaluated is not increased.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The Emergency Diesel Generator system is not an accident 
    initiator. The operation and design of the onsite emergency power 
    system (including the EDGs) is not being changed; only the overhaul 
    inspection interval coupled with the program improvements and the 
    corresponding interval change for the associated 24 hour endurance 
    test and hot restart test, (which are normally performed in 
    conjunction with the diesel preventive maintenance overhaul 
    inspections), are changed. The EDG system meets the single failure 
    criteria at the EDG unit level, i.e., the SAR [safety analysis 
    report] states that with one EDG failed or out-of-service, the 
    standby AC system is capable of furnishing sufficient power for the 
    minimum Class 1E load demand, assuming a limiting design basis 
    accident has occurred. The proposed changes involve a routine 
    preventive maintenance and inspection time interval change along 
    with the corresponding surveillance test interval changes, and also 
    include programmatic improvements to reduce the likelihood of a 
    failure of an individual EDG unit; the proposed changes do not 
    involve any physical design or operational changes that could create 
    a malfunction extending beyond an individual EDG nor do they 
    increase the potential for a common-mode EDG failure. Therefore, it 
    is not possible to create a new or different type of accident 
    through implementation of these changes.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The changes to bring the frequencies of the EDG overhaul, the 24 
    hour endurance test and the associated hot restart test into 
    alignment with the current 2 year operating cycle, and the detailed 
    programmatic changes to achieve conformance with the FMOG [Fairbanks 
    Morse Owners Group] recommended maintenance program, will increase 
    the reliability and availability of the EDG system. This will 
    enhance the margin of safety as the amount of time the EDGs are out-
    of-service will decrease and the system will be single-failure proof 
    for more clock hours when the nuclear reactor(s) are operating. The 
    changes discussed here do not result in operation of the emergency 
    diesel generator system nor any other plant system in a manner 
    beyond their original design basis, and thus does not reduce any 
    explicit or implicit Technical Specification margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101.
        NRC Project Director: William M. Dean.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: February 12, 1997.
        Brief description of amendment: The proposed amendment would delete 
    a portion of the Trojan site from the 10 CFR 50 license when that 
    portion of the site, designated for use as an independently licensed 
    spent fuel storage installation (ISFSI), receives a part 72 license.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensees' analysis 
    against the standards of 10 CFR 50.92(c). The licensee's analysis is 
    summarized below:
        The proposed changes would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The proposed change is administrative in nature and has no impact on 
    the probability or consequences of accidents previously evaluated. The 
    physical structures, systems, and components of the Trojan Nuclear 
    Plant and the operating procedures for their use are unaffected by this 
    proposed change. The proposed action would eliminate the ISFSI area 
    from the Part 50 license when the Part 72 license is issued. The 10 CFR 
    72 licensing controls for the area will assure an adequate level of 
    safety for the area during normal operation of the ISFSI and during 
    abnormal events or accidents. Therefore the proposed Part 50 amendment 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. The 
    proposed action would eliminate the ISFSI area from the Part 50 license 
    when the Part 72 license is issued. The proposed change is 
    administrative in
    
    [[Page 9197]]
    
    nature and has no impact on plant systems, structures, or components or 
    on any procedures for operating the plant equipment. The ISFSI will be 
    separately licensed under Part 72 and physically separated from the 
    Part 50 licensed structures and equipment. Therefore, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from those previously evaluated.
        The proposed changes do not involve reduction in the margin of 
    safety. The Trojan Permanently Defueled Technical Specifications (PDTS) 
    contain four limiting conditions of operation that address: 1) Spent 
    Fuel Water Level, 2) Spent Fuel Pool Boron Concentration, 3) Spent Fuel 
    Pool Temperature, and 4) Spent Fuel Pool load restrictions. These PDTS 
    will remain in effect as long as spent fuel is stored in the Spent Fuel 
    Pool, which is in accordance with their applicability statements. The 
    ISFSI area is physically separated from the Spent Fuel Pool area and 
    the Fuel Building and will have no effect on spent fuel water level, 
    spent fuel pool boron concentration, spent fuel pool temperature, or 
    loads over the Spent Fuel Pool. The proposed change is administrative 
    and does not affect plant equipment, operating parameters, or 
    procedures. Based on the above, the proposed change will not reduce the 
    margin of safety.
        Based on a staff review of the licensee's analysis, it appears that 
    the three standards of 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
        Attorney for licensees: Leonard A. Girard, Esq., Portland General 
    Electric Company, 121 S. W. Salmon Street, Portland, Oregon 97204.
        NRR Project Director: Seymour H. Weiss.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: January 7, 1999.
        Brief description of amendment: The proposed amendment would allow 
    loading and handling of spent fuel transfer and storage casks in the 
    Trojan Fuel Building.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensees' analysis 
    against the standards of 10 CFR 50.92(c). The licensee's analysis is 
    summarized below:
        The proposed changes would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    With the permanent cessation of operations, the number of potential 
    accidents was reduced to those types of accidents associated with the 
    storage of irradiated fuel and radioactive waste storage and handling. 
    Additional events were postulated for decommissioning activities due to 
    the difference in the types of activities that were to be performed. 
    The postulated accidents in the Defueled Safety Analysis Report (DSAR) 
    are generally classified as: (1) radioactive release from a subsystem 
    or component, (2) fuel handling accident and, (3) loss of spent fuel 
    decay heat removal capability. The postulated events described in the 
    Decommissioning Plan are grouped as: (1) decontamination, 
    dismantlement, and materials handling events, (2) loss of support 
    systems (offsite power, cooling water, and compressed air), (3) fire 
    and explosions, and (4) external events (earthquake, external flooding, 
    tornadoes, extreme winds, volcanoes, lightning, toxic chemical 
    release). These types of accidents are discussed below.
        Radioactive release from a subsystem or component involves failure 
    of a radioactive waste gas decay tank (WGDT) or failure of a chemical 
    and volume control system holdup tank (HUT). For a failure of a WGDT, 
    the radioactive contents are assumed to be principally the noble gases 
    krypton and xenon, the particulate daughters of some of the krypton and 
    xenon isotopes and trace quantities of halogens. For the failure of a 
    HUT, the assumptions were full power operations with 1-percent failed 
    fuel, 40 weeks elapsed since power operation, and 60,000 gallons of 
    120 deg. F liquid released over a 2-hour period. However, the WGDT's 
    and HUT's are no longer active and have been emptied. Therefore, cask 
    loading and transfer activities cannot increase the probability of 
    occurrence of a failure or the consequence of a failure of the WGDT's 
    or HUT's.
        The fuel handling accident involves a stuck or dropped fuel 
    assembly that results in damage of the cladding of the fuel rods in one 
    assembly and the release of gaseous fission products. Spent fuel 
    handling and loading will involve moving the spent fuel assemblies one 
    by one, from the Spent Fuel Pool to the baskets which will be located 
    in the Cask Loading Pit. The fuel handling equipment will be the same 
    as had been previously analyzed with the exception of special tools 
    which will be used to manipulate failed fuel. These special tools will 
    be similar in size and weight to the existing tools used for underwater 
    manipulation and therefore will not present a new hazard. In addition, 
    the same administrative controls and physical limitations imposed on 
    any fuel handling operation will be used for spent fuel loading and 
    handling. The potential release, 100 percent of gap noble gas, from a 
    fuel assembly is not affected (although the fission product inventory 
    in a fuel assembly continues to decrease with time). Thus there is no 
    increase in the probability of occurrence or consequences of a fuel 
    handling accident over what would be expected for any routine fuel 
    handling operation.
        The loss of spent fuel decay heat removal capability involves the 
    loss of forced spent fuel cooling with and without concurrent Spent 
    Fuel Pool inventory loss. The only requirement to assure adequate decay 
    heat removal capability for the spent fuel is to maintain the water 
    level in the Spent Fuel Pool so that the fuel assemblies remain covered 
    (i.e. the capability to make up water to the Spent Fuel Pool must be 
    available when required). The potential events which could result in a 
    loss of spent fuel decay heat removal include external events 
    (explosions, toxic chemical, fires, ship collision with intake 
    structure, oil or corrosive liquid spills in the river, cooling tower 
    collapse, seismic events, severe meteorological events), and internal 
    events including Spent Fuel Pool makeup water system malfunctions 
    (Service Water System, electrical power, instrument air). Spent fuel 
    loading and handling will not require the use of explosive materials 
    (the gases used for electric arc welding are inert), toxic chemicals or 
    flammable materials (routine use of contamination control materials is 
    not considered to present a significant hazard). The probability of 
    other external events (e.g. cooling tower collapse) is not effected by 
    the spent fuel handling and loading activities inside the Fuel 
    Building. Spent fuel loading and handling activities will not directly 
    interface with the Spent Fuel Pool makeup water systems, therefore does 
    not affect their probability of failure. (The Cask Loading Pit will be 
    filled with borated water from the Spent Fuel Pool that will be cooled 
    by the Spent Fuel Cooling System, but use of this water in the Cask 
    Loading Pit does not increase the failure probability of
    
    [[Page 9198]]
    
    the Spent Fuel Pool or makeup water systems.) As described in the 
    licensees' safety evaluation, the safe load path and handling height 
    limitations will ensure that a load drop does not adversely affect the 
    Spent Fuel Pool or the makeup water systems. Therefore there is no 
    significant increase in the probability or consequences of a loss of 
    spent fuel decay heat removal capability.
        The events postulated in the Decommissioning Plan are similar to 
    the DSAR with the exception of the decontamination, dismantlement, and 
    materials handling events. Decontamination events involve gross liquid 
    leakage from in-situ decontamination equipment (e.g. tanks) or 
    accidental spraying of liquids containing concentrated contamination. 
    Dismantlement events involve segmentation of components and structures, 
    or removal of concrete by rock splitting, explosives, or electric and/
    or pneumatic hammers. Dismantlement events potentially result in 
    airborne contamination. Material handling events involve the dropping 
    of contaminated components, concrete rubble, filters, or packages of 
    particulate materials. Licensee administrative controls will be 
    implemented to ensure that spent fuel loading and handling activities 
    and decommissioning activities will not be performed concurrently if 
    they interact with each other and could increase the probability or 
    consequences of a postulated event of accident. Therefore, neither the 
    probability nor the consequences of decontamination, dismantlement, and 
    materials handling events will not be significantly increased.
        The proposed changes would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. As 
    described in the licensees' safety evaluation the potential accidents 
    associated with fuel handling and loading were similar to fuel handling 
    accidents, material handling events and pressurized line break 
    previously analyzed. Additionally the potential consequences were a 
    small fraction of Environmental Protection Agency (EPA) Protective 
    Action Guides (PAG's). Therefore, fuel loading and handling does not 
    present new or different types of accidents.
        The proposed changes do not involve a significant reduction in the 
    margin of safety. The Trojan Permanently Defueled Technical 
    Specifications (PDTS) contain four limiting conditions of operation 
    that address: (1) Spent fuel water level, (2) spent fuel pool boron 
    concentration, (3) spent fuel pool temperature, and (4) spent fuel pool 
    load restrictions. These PDTS will remain in effect as long as spent 
    fuel is stored in the Spent Fuel Pool, which is in accordance with 
    their applicability statements. The spent fuel loading and handling 
    activities will not affect these PDTS or their bases.
        The Cask Loading Pit, where the spent fuel will be loaded into the 
    basket, is immediately adjacent to the Spent Fuel Pool. The gate 
    between the Cask Loading Pit and Spent Fuel Pool will be open to allow 
    transfer of spent fuel assemblies from storage racks in the Spent Fuel 
    Pool to the basket in the Cask Loading Pit. Opening the gate between 
    them will allow free exchange of water between the Cask Loading Pit and 
    the Spent Fuel Pool. The Cask Loading Pit will be filled with borated 
    water at approximately the same concentration and temperature as the 
    Spent Fuel Pool prior to opening the gate. This will maintain the 
    limiting conditions for operation for Spent Fuel Pool boron 
    concentration, temperature, and water level and the margin of safety 
    will not be affected.
        Spent fuel loading and handling activities will involve lifting and 
    moving heavy loads (e.g. transfer cask, basket). Loads that will be 
    carried over fuel in the Spent Fuel Pool racks and the heights at which 
    they will be carried will be limited to preclude impact energies over 
    240,000 in-lbs if the loads were dropped. This is in accordance with 
    limiting condition for operation 3.1.4 ``Spent Fuel Pool Load 
    Restrictions.'' With this precaution, the limiting condition for 
    operation pertaining to load restrictions over the Spent Fuel Pool will 
    be satisfied and the margin of safety will be unaffected. The safe load 
    paths for heavy loads being lifted outside the Spent Fuel Pool will be 
    sufficiently far from the Spent Fuel Pool so as to not have an 
    interaction in the unlikely event of a load drop. In addition 
    mechanical stops and electrical interlocks on the Fuel Building 
    overhead crane will provide additional assurance that heavy loads are 
    not carried over the Spent Fuel Pool racks.
        Based on the above, the spent fuel loading and handling activities 
    will not reduce the margin of safety.
        Based on a staff review of the licensee's analysis, it appears that 
    the three standards of 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
        Attorney for licensees: Leonard A. Girard, Esq., Portland General 
    Electric Company, 121 S. W. Salmon Street, Portland, Oregon 97204.
        NRR Project Director: Seymour H. Weiss.
    
    Portland General Electric Company, et l., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: January 27, 1999.
        Brief description of amendment: The proposed amendment would allow 
    unloading of spent fuel transfer casks in the Trojan Fuel Building.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The licensee's analysis is 
    summarized below:
        The proposed changes would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    With the permanent cessation of operations, the number of potential 
    accidents was reduced to those types of accidents associated with the 
    storage of irradiated fuel and radioactive waste storage and handling. 
    Additional events were postulated for decommissioning activities due to 
    the difference in the types of activities that were to be performed. 
    The postulated accidents in the Defueled Safety Analysis Report (DSAR) 
    are generally classified as: (1) Radioactive release from a subsystem 
    or component, (2) fuel handling accident and, (3) loss of spent fuel 
    decay heat removal capability. The postulated events described in the 
    Decommissioning Plan are grouped as: (1) Decontamination, 
    dismantlement, and materials handling events, (2) loss of support 
    systems (offsite power, cooling water, and compressed air), (3) fire 
    and explosions, and (4) external events (earthquake, external flooding, 
    tornadoes, extreme winds, volcanoes, lightning, and toxic chemical 
    release). These types of accidents are discussed below.
        Radioactive release from a subsystem or component involves failure 
    of a radioactive waste gas decay tank (WGDT) or failure of a chemical 
    and volume control system holdup tank (HUT). For a failure of a WGDT, 
    the radioactive contents are assumed to be principally the noble gases 
    krypton and xenon, the particulate daughters of some
    
    [[Page 9199]]
    
    of the krypton and xenon isotopes and trace quantities of halogens. For 
    the failure of a HUT, the assumptions were full power operations with 
    1-percent failed fuel, 40 weeks elapsed since power operation, and 
    60,000 gallons of 120 deg. F liquid released over a two hour period. 
    However, the WGDT's and HUT's are no longer active and have been 
    emptied. Therefore, cask loading and transfer activities cannot 
    increase the probability of occurrence of a failure or the consequence 
    of a failure of the WGDT's or HUT's.
        The fuel handling accident involves a stuck or dropped fuel 
    assembly that results in damage of the cladding of the fuel rods in one 
    assembly and the release of gaseous fission products. Spent fuel cask 
    unloading will involve moving the spent fuel assemblies one by one, 
    from the baskets which will be located in the cask loading pit to the 
    spent fuel pool. The fuel handling equipment will be the same as had 
    been previously analyzed. In addition, the same administrative controls 
    on physical limitations imposed on fuel handling and fuel loading 
    operations will be used for fuel unloading. The potential release, 100 
    percent of noble gases within the gap, from a fuel assembly is not 
    affected (although the inventory in a radioactive stored fuel assembly 
    continues to decrease with time). Thus, there is no increase in the 
    probability of occurrence or consequences of a fuel handling accident 
    over what would be expected for any routine fuel handling operation or 
    loading of fuel into a cask.
        The loss of spent fuel decay heat removal capability involves the 
    loss of forced spent fuel cooling with and without concurrent spent 
    fuel pool inventory loss. The only requirement to assure adequate decay 
    heat removal capability for the spent fuel is to maintain the water 
    level in the spent fuel pool so that the fuel assemblies remain covered 
    (i.e., the capability to make up water to the spent fuel pool must be 
    available when required). The potential events that could result in a 
    loss of spent fuel decay heat removal include external events 
    (explosions, toxic chemical, fires, ship collision with intake 
    structure, oil or corrosive liquid spills in the river, cooling tower 
    collapse, seismic events, and severe meteorological events), and 
    internal events including spent fuel pool makeup water system 
    malfunctions (service water system, electrical power, and instrument 
    air). Spent fuel cask unloading will not require the use of explosive 
    materials, toxic chemicals or flammable materials (routine use of 
    contamination control materials is not considered to present a 
    significant hazard). The probability of other external events (e.g. 
    cooling tower collapse) is not effected by the spent fuel unloading 
    activities inside the fuel building. Spent fuel cask unloading 
    activities will not directly interface with the spent fuel pool makeup 
    water systems, and therefore does not affect their probability of 
    failure. (The cask loading pit will be filled with borated water from 
    the spent fuel pool that will be cooled by the spent fuel cooling 
    system, but use of this water in the cask loading pit does not increase 
    the failure probability of the spent fuel pool or makeup water 
    systems). As described in the licensees' safety evaluation, the safe 
    load path and handling height limitations will ensure that a load drop 
    does not adversely affect the spent fuel pool or the makeup water 
    systems. Therefore, there is no significant increase in the probability 
    or consequences of a loss of spent fuel decay heat removal capability.
        The events postulated in the Decommissioning Plan are similar to 
    the DSAR with the exception of the decontamination, dismantlement, and 
    materials handling events. Decontamination events involve gross liquid 
    leakage from in-situ decontamination equipment (e.g. tanks) or 
    accidental spraying of liquids containing concentrated contamination. 
    Dismantlement events involve segmentation of components and structures, 
    or removal of concrete by rock splitting, explosives, or electric and/
    or pneumatic hammers. Dismantlement events potentially result in 
    airborne contamination. Material handling events involve the dropping 
    of contaminated components, concrete rubble, filters, or packages of 
    particulate materials. Licensee administrative controls will be 
    implemented to ensure that spent fuel cask unloading activities and 
    decommissioning activities will not be performed concurrently if they 
    interact with each other and could increase the probability or 
    consequences of a postulated event of accident. Therefore, neither the 
    probability nor the consequences of decontamination, dismantlement, and 
    materials handling events will be significantly increased.
        The proposed changes would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. As 
    described in the licensee's safety evaluation the potential accidents 
    associated with fuel cask unloading were similar to fuel handling 
    accidents, material handling events and pressurized line break 
    previously analyzed. Additionally the potential consequences were a 
    small fraction of Environmental Protection Agency (EPA) Protective 
    Action Guides (PAGs). Therefore, fuel loading and handling does not 
    present new or different types of accidents.
        The proposed changes do not involve a significant reduction in the 
    margin of safety. The Trojan Permanently Defueled Technical 
    Specifications (PDTS) contain four limiting conditions of operation 
    that address: (1) spent fuel pool water level, (2) spent fuel pool 
    boron concentration, (3) spent fuel pool temperature, and (4) spent 
    fuel pool load restrictions. These PDTS will remain in effect as long 
    as spent fuel is stored in the spent fuel pool, which is in accordance 
    with their applicability statements. The spent fuel cask unloading 
    activities will not affect these PDTS or their bases.
        The cask loading pit, where the spent fuel will be unloaded from 
    basket, is immediately adjacent to the spent fuel pool. The gate 
    between the cask loading pit and spent fuel pool will be open to allow 
    transfer of spent fuel assemblies from the basket in the cask loading 
    pit to the storage racks in the spent fuel pool. Opening the gate 
    between them will allow free exchange of water between the cask loading 
    pit and the spent fuel pool. The cask loading pit will be filled with 
    borated water at approximately the same concentration and temperature 
    as the spent fuel pool prior to initial cask loading. This will 
    maintain the limiting conditions for operation for spent fuel pool 
    boron concentration, temperature, and water level and the margin of 
    safety will not be affected.
        Spent fuel cask unloading activities may involve lifting and moving 
    heavy loads (e.g. transfer cask, basket). Loads that will be carried 
    over fuel in the spent fuel pool racks and the heights at which they 
    will be carried will be limited to preclude impact energies over 
    240,000 in-lbs if the loads were dropped. This is in accordance with 
    limiting condition for operation 3.1.4 ``Spent Fuel Pool Load 
    Restrictions.'' With this precaution, the limiting condition for 
    operation pertaining to load restrictions over the spent fuel pool will 
    be satisfied and the margin of safety will be unaffected. The safe load 
    paths for heavy loads being lifted outside the spent fuel pool will be 
    sufficiently far from the spent fuel pool so as to not have an 
    interaction in the unlikely event of a load drop. In addition, 
    mechanical stops and electrical interlocks on the fuel building 
    overhead crane will provide additional assurance that heavy loads are 
    not carried over the spent fuel pool racks.
    
    [[Page 9200]]
    
        Based on the above, the spent fuel cask unloading activities will 
    not reduce the margin of safety.
        Based on a staff review of the licensee's analysis, it appears that 
    the three standards of 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
        Attorney for licensees: Leonard A. Girard, Esq., Portland General 
    Electric Company, 121 S.W. Salmon Street, Portland, Oregon 97204.
        NRR Project Director: Seymour H. Weiss.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: October 16, 1998, as supplemented 
    January 28, 1999.
        Description of amendment request: This application for amendment to 
    the Indian Point 3 (IP3) Technical Specifications (TSs) proposes to 
    relocate the Chemical Volume and Control System (CVCS) TS 3.2 from the 
    TSs to the IP3 Operational Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed?
        Response: Relocation (i.e., removal from TS) of TS 3.2, the 
    bases and the associated surveillances in Table 4.1-1 (items 12, 26, 
    and 27), Table 4.1-2 (item 2), and Table 4.1-3 (item 12) will not 
    involve a significant increase [in] the probability or consequences 
    of an accident since the relocation of the Technical Specifications 
    to administrative controls governed by 10 CFR 50.59 does not affect 
    the availability or function of charging and boric acid flow paths. 
    CVCS is not an initiator of an accident (the dilution event is 
    equipment malfunction that is manually terminated) and the proposed 
    change does not alter overall system operation, physical design, 
    system configuration, or operational setpoints. There will be no 
    significant increase in the consequences of an accident because the 
    required boration flow paths will continue to be available for 
    boration to the reactor coolant system.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response: Relocation (i.e., removal from TS) of TS 3.2, the 
    bases and the associated surveillances in Table 4.1-1 (items 12, 26, 
    and 27), Table 4.1-2 (item 2), and Table 4.1-3 (item 12) will not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated since it does not alter the overall system 
    operation, physical design, system configuration, or operational 
    setpoints. The plant systems for boration are operated in the same 
    manner as before and, consequently, the relocation does not 
    introduce any new accident initiators or failure mechanisms and does 
    not invalidate the existing dilution event response. The boration 
    function is not an accident initiator.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response: Relocation (i.e., removal from TS) of TS 3.2, the 
    bases and the associated surveillances in Table 4.1-1 (items 12, 26, 
    and 27), Table 4.1-2 (item 2), and Table 4.1-3 (item 12) will not 
    involve a significant reduction in margin of safety. The relocation 
    is a change to the administrative controls that are used to assure 
    system availability and those administrative controls are governed 
    by 10 CFR 50.59. The manner in which the system is operated does not 
    change and there is no change to physical design, system 
    configuration, or operational setpoints. Previous analyses of system 
    malfunction remain unchanged. The current Technical Specification 
    does not meet the criteria in 10 CFR 50.36(c)(2)(ii) for inclusion 
    in the technical specifications.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. David E. Blabey, 10 Columbus Circle, New 
    York, New York 10019.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of amendment request: December 30, 1998.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Limiting Condition for Operation 
    (LCO) 3.7.3 and Table 3.7.3-1. The proposed changes would modify the 
    flood protection actions required during periods of elevated river 
    water level.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed TS revisions related to flood protection TS Action 
    Statements involve no hardware changes and no changes to existing 
    structures, systems or components. The proposed changes to the flood 
    protection TS Action Statements ensure that the supported systems 
    can perform their required safety functions under worst case design 
    basis conditions, consistent with limitations imposed by other TS. 
    The proposed flood protection TS ACTION Statements ensure that the 
    plant is directed to enter a safe shutdown condition whenever the 
    capability to withstand worst case design basis conditions is 
    affected. Since the flood protection changes will still ensure that 
    the plant remains capable of meeting applicable design basis 
    requirements and retains the capability to mitigate the consequences 
    of accidents described in the [Hope Creek] HC [Updated Final Safety 
    Analysis Report] UFSAR, the proposed changes were determined to be 
    acceptable. As a result, these changes will neither increase the 
    probability of an accident previously evaluated nor increase the 
    radiological dose consequences of an accident previously evaluated.
        (2) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the flood protection TS contained in 
    this submittal will not adversely impact the operation of any safety 
    related component or equipment. Since the proposed changes involve 
    no hardware changes and no changes to existing structures, systems 
    or components, there can be no impact on the potential occurrence of 
    any accident due to new equipment failure modes. The resulting 
    operational limits imposed by the flood protection LCO ensure that 
    the plant can either perform its design basis safety functions or an 
    appropriately conservative shutdown action statement is entered. 
    Furthermore, there is no change in plant testing proposed in this 
    change request that could initiate an event. Therefore, these 
    changes will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        (3) The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes for the flood protection TS retain the 
    plant's continued capability to withstand worst case design basis 
    conditions. The proposed flood protection TS ACTION Statements 
    ensure that the plant is directed to: (1) enter a safe shutdown 
    condition whenever the capability to withstand worst case design 
    basis conditions is lost; or (2) enter a conservatively short period 
    of continued operation when supported system redundancy is reduced. 
    Since the plant will still remain capable of meeting all applicable 
    design basis requirements and retaining the
    
    [[Page 9201]]
    
    capability to withstand worst case design basis events described in 
    the HC UFSAR, the proposed changes were determined to not result in 
    a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Project Director: William M. Dean.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Description of amendment request: The proposed changes revise the 
    descriptive details of Technical Specification 4.7.1.2.1.a, regarding 
    performance testing of the Auxiliary Feedwater (AFW) pumps, to more 
    closely adhere to NUREG-1431, Improved Standard Technical 
    Specifications for Westinghouse Plants. This involves relocating the 
    surveillance-required numerical values for the AFW pump performance 
    test discharge pressure and flow rate to the South Texas Project 
    Updated Final Safety Analysis Report (UFSAR).
        Date of amendment request: January 20, 1999.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change, which relocates descriptive details (i.e., 
    numerical values for AFW pump discharge pressure and flow rate) of 
    the surveillance testing applicable to the AFW pumps, does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated. The affected AFW pump testing 
    pressure and flow descriptive details that are being removed from 
    SRs 4.7.1.2.1.a.1 and 4.7.1.2.1.a.2 are not related to any assumed 
    initiators of analyzed events and are not assumed to mitigate 
    accident or transient events. The requirement to perform testing on 
    a monthly, staggered basis is not altered by the proposed change, 
    and will remain in the Technical Specifications. The descriptive 
    details of the surveillance testing will be relocated from the 
    Technical Specifications to the USFAR and will be maintained 
    pursuant to 10CFR50.59. The proposed revised wording of SRs 
    4.7.1.2.1.a.1 and 4.7.1.2.1.a.2 (i.e., to verify the developed head 
    of each pump is greater than or equal to the required developed 
    head) and the relocation of pump testing details to the UFSAR is 
    consistent with the AFW pump test requirements in NUREG-1431. In 
    addition, the surveillance testing details are addressed in existing 
    surveillance procedures that are also controlled by 10CFR50.59 and 
    subject to the change control provisions imposed by plant 
    administrative procedures, which endorse applicable regulations and 
    standards. Therefore, this proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change relocates descriptive details (i.e., 
    numerical values for AFW pump discharge pressure and flow rate) of 
    surveillance testing applicable to the AFW pumps, which do not meet 
    the criteria for inclusion in Technical Specifications as identified 
    in 10CFR50.36(c)(3). The requirement to perform testing on a 
    monthly, staggered basis is not altered by the proposed change, and 
    will remain in the Technical Specifications. Additionally, 
    relocation of the descriptive testing details is consistent with the 
    wording of the AFW pump test requirements in NUREG-1431, which does 
    not specify minimum numerical pressure and flow limits. The proposed 
    change does not involve a physical alteration of the plant (no new 
    or different type of equipment will be installed) or make changes in 
    the methods governing normal plant operation. The change will not 
    impose different requirements, and any future changes to these 
    relocated surveillance testing details or to the applicable 
    surveillance procedures will be evaluated per the requirements of 
    10CFR50.59. This change will not alter assumptions made in the 
    safety analysis and licensing basis. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change, which relocates descriptive details (i.e., 
    numerical values for AFW pump discharge pressure and flow rate) of 
    the surveillance testing applicable to the AFW pumps, will not 
    reduce a margin of safety since it has no impact on any safety 
    analysis assumptions. The requirement to perform AFW pump testing on 
    a monthly, staggered basis will not be altered by the proposed 
    change, and will remain in the Technical Specifications. 
    Furthermore, the proposed change will not affect the operability 
    requirements of the AFW system as delineated in Specification 
    3.7.1.2. Since any future changes to these relocated surveillance 
    testing details or to the applicable surveillance procedures will be 
    evaluated per the requirements of 10CFR50.59, there is no reduction 
    in a margin of safety. Finally, this proposed change is also 
    consistent with NUREG-1431, previously approved by the NRC Staff. 
    Revising the Technical Specifications to reflect the approved NUREG-
    1431 content ensures no significant reduction in the margin of 
    safety. Therefore, this proposed change does not involve a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869.
        NRC Project Director: John N. Hannon.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: January 15, 1999 (TS 98-07).
        Brief description of amendments: The proposed amendments would 
    change the Sequoyah (SQN) Technical Specification (TS) requirements by 
    adding a new action statement to TS 3.1.3.2, ``Position Indicating 
    Systems--Operating,'' that eliminates the need to enter TS 3.0.3 
    whenever two or more individual rod position indicators (RPIs) may be 
    inoperable per bank, while maintaining the appropriate overall level of 
    protection and adding flexibility to the initial determination of the 
    position of the non-indicating rod(s).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority (TVA), the licensee, has provided its analysis of the issue 
    of no significant hazards consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change to TS 3.1.3.2 does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The potential for the new action statement to 
    impact the probability or consequences of the safety analyses for 
    the plant lies only in the area of operator-exacerbated reactivity 
    events due to
    
    [[Page 9202]]
    
    a loss of RCCA [rod control cluster assembly] position indication.
        RCCA events such as: One or more dropped RCCAs, a dropped RCCA 
    bank or a RCCA ejection (FSAR [Final Safety Analysis Report] 
    Sections 15.2.3 and 15.4.6, respectively) are not impacted since the 
    new action statement does not involve a design change. Events such 
    as: Uncontrolled RCCA bank withdrawal at power, statically 
    misaligned RCCA or withdrawal of a single RCCA (FSAR Sections 
    15.2.2, 15.2.3, and 15.3.6, respectively) involve, or potentially 
    involve, operator action and are of interest. The uncontrolled RCCA 
    bank withdrawal at power is an ANS [American Nuclear Society] 
    Condition II transient that has been analyzed using a positive 
    reactivity insertion rate greater than that for the simultaneous 
    withdrawal of the two control banks having the maximum combined 
    worth at maximum speed. Whether the event is caused by a failure in 
    the rod control system or by operator error has no effect on the 
    positive reactivity insertion rate assumed in the analysis. The 
    protection systems assumed in the analysis are unaffected since 
    there is no change to the design. Loss of the RPIS would not result 
    in more frequent control rod movement by plant operators. Therefore, 
    the new action statement would not affect the analysis of this event 
    and departure from nucleate boiling ratio (DNBR) design basis would 
    still be met.
        The most severe misalignment situation, with respect to DNBR, 
    arises from cases in which one RCCA is fully inserted or where Bank 
    D is fully inserted to its insertion limits with one RCCA fully 
    withdrawn. For these cases, as discussed in FSAR Section 15.2.3.2, 
    the DNBR remains above the safety analysis limit values. Also, the 
    control bank insertion limit alarms remain available to warn 
    operators that bank insertion limits have been reached.
        A compensatory action associated with this new action statement, 
    placing the control rods under manual control, addresses concerns 
    associated with automatic rod motion due to the rod control system 
    and inadvertent operator contribution to these events.
        The worst-case event of those described above, the withdrawal of 
    a single RCCA, is an ANS Condition III event. It has been analyzed 
    in FSAR Section 15.3.6, assuming that operators ignore RCCA position 
    indication or that multiple rod control system failures occur. No 
    single electrical or mechanical failure in the rod control system 
    could cause the accidental withdrawal of a single RCCA from an 
    inserted bank at full power operation. The operator could 
    deliberately withdraw a single RCCA in the control bank. This 
    feature is necessary in order to retrieve an accidentally dropped 
    rod. This new action statement does not change the plant design; 
    therefore, there would be no change in the probability of the event 
    being induced by the unlikely, simultaneous electrical failures 
    (FSAR Section 7.7.2.2).
        The change in the time to determine the position of the non-
    indicating rods, indirectly with the movable incore detectors, does 
    not involve a design change nor does it affect the immediate 
    response of the operator to the event, therefore, it does not affect 
    the results of the analyses described above.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Since there is no change to the design associated with the 
    proposed change, it does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The proposed change involves a loss of the RPIS [Rod Position 
    Indication System] and establishes compensatory measures to maintain 
    control rod position consistent with the assumptions used in the 
    existing accident and transient analyses. The new action statement 
    provides sufficient time for troubleshooting while avoiding 
    unnecessary plant shutdowns per TS 3.0.3.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed change to TS 3.1.3.2 does not involve a significant 
    reduction in a margin of safety. As discussed in Section IV.A above, 
    the results of the FSAR Chapter 15 safety analyses for the 
    applicable events, are not affected by the proposed changes. 
    Therefore, the safety margins demonstrated by these analyses remain 
    unchanged. The additional time to obtain the flux maps is consistent 
    with the 12-hour time frame allowed to verify shutdown margin when a 
    rod is misaligned from its group step counter height by more than 
    plus or minus 12 steps in TS 3.1.3.1 and remains within a shiftly 
    basis. Therefore, it does not reduce the margin of safety.
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Project Director: Cecil O. Thomas.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: January 29, 1999 (TSCR 211).
        Description of amendment request: The proposed amendments reflect 
    changes to sections 15.6 and 15.7 of the Point Beach Nuclear Plant 
    (PBNP), Units 1 and 2, Technical Specifications (TS). The proposed 
    changes are considered administrative in nature and reflect personnel 
    title changes, an increase in minimum operating crew shift staffing, 
    relocation of the Manager's Supervisory Staff composition and 
    functional requirements to owner controlled documents, and revisions to 
    the procedure review and approval process.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not result in a significant increase in 
    the probability or consequences of an accident previously evaluated.
        These changes are administrative and therefore do not involve a 
    significant increase in the probability of an accident previously 
    evaluated because no such accidents are affected by the proposed 
    revisions. The proposed TS changes do not introduce any new accident 
    initiators since no accidents previously evaluated have as their 
    initiators anything related to the administrative changes described 
    above.
        In addition, initiating conditions and assumptions are unchanged 
    and remain as previously analyzed for accidents in the PBNP Final 
    Safety Analysis Report. The proposed TS changes do not involve any 
    physical changes to systems or components, nor do they alter the 
    typical manner in which the systems or components are operated. All 
    Limiting Conditions [for] Operation, Limiting Safety System 
    Settings, and Safety Limits specified in the TS remain unchanged. 
    Therefore, these changes do not increase the probability of 
    previously evaluated accidents.
        These changes do not involve a significant increase in the 
    consequences of an accident previously evaluated because the source 
    term, containment isolation or radiological releases are not being 
    changed by these proposed revisions. Existing system and component 
    redundancy and operation is not being changed by these proposed 
    changes. The assumptions used in evaluating the radiological 
    consequences in the PBNP Final Safety Analysis Report are not 
    invalidated; therefore, these changes do not affect the consequences 
    of previously evaluated accidents.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        These changes do not introduce nor increase the number of 
    failure mechanisms of a new or different type than those previously 
    evaluated since there are no physical changes being made to the 
    facility. The design and design basis of the facility remain 
    unchanged. The plant safety analyses remain unchanged. Therefore, 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated is not introduced.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not involve a significant reduction in 
    a margin of safety.
    
    [[Page 9203]]
    
        The proposed changes do not involve a significant reduction in 
    the margin of safety because existing component redundancy is not 
    being changed by these proposed changes. There are no new or 
    significant changes to the initial conditions contributing to 
    accident severity or consequences, and safety margins established 
    through the design and facility license including the Technical 
    Specifications remain unchanged. Therefore, there are no significant 
    reductions in a margin of safety introduced by [these] proposed 
    amendment[s].
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: December 29, 1998.
        Description of amendment request: This amendment would revise the 
    Wolf Creek Technical Specification (TS) Figures 3.4-2, 3.4-3, and 3.4-4 
    to incorporate revised reactor coolant system heatup and cooldown limit 
    curves and a revised cold overpressure mitigation system (COMS) power 
    operated relief valve (PORV) setpoint limit curve.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Incorporating the revised heatup and cooldown pressure/
    temperature limit curves and the COMS PORV setpoint limit curve into 
    the WCGS Technical Specifications does not affect the probability or 
    consequences of an accident previously evaluated.
        The revised limit curves are calculated using the most limiting 
    RTNDT for the reactor vessel components and include a 
    radiation-induced shift corresponding to the end of the period for 
    which the curves are generated. The COMS PORV Setpoint Limit Curve 
    is calculated using the most limiting mass injection transient, 
    taking into account operation of the NCP [normal charging pump] 
    during shutdown modes. The changes do not affect the basis, 
    initiating events, chronology, or availability/operability of safety 
    related equipment required to mitigate transients and accidents 
    analyzed for WCGS.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Adopting the revised limit curves redefines the range of 
    acceptable operation for the Reactor Coolant System. This 
    redefinition is a result of the analysis of reactor vessel 
    surveillance specimens removed from the reactor in a continuing 
    surveillance program which monitors the effects of neutron 
    irradiation on the WCGS reactor vessel materials under actual 
    operating conditions. Included in the revised limit curves is 
    consideration for NCP operation during shutdown modes. Incorporating 
    these revised curves does not create the possibility of an accident 
    of a different type from any previously evaluated for WCGS.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The revision of these limit curves continues to maintain the 
    margin of safety required for prevention of non-ductile failure of 
    the WCGS reactor vessel during low temperature operation as required 
    by 10 CFR 50, Appendices G and H. The revised curves primarily 
    affect RCS [reactor coolant system] operation below 350 deg.F by 
    limiting the available pressure/temperature window for heatup and 
    cooldown. The revised limit curves compensate for the in-service 
    radiation induced embrittlement of the reactor vessel and accounts 
    for the requirement that the closure flange region temperature must 
    exceed the nil-ductility temperature by at least 120 deg.F when 
    pressure exceeds 20% of the preservice hydrostatic test pressure.
        The revised COMS PORV Setpoint Limit Curve, which includes 
    consideration of NCP operation during shutdown modes, ensures 
    overpressure protection of the RCS and reactor vessel.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037.
        NRC Project Director: William H. Bateman.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: January 12, 1999.
        Description of amendment request: This license amendment request 
    proposes to revise Wolf Creek Generating Station (WCGS) Technical 
    Specification 3/4.7.5, Ultimate Heat Sink, to add a new action 
    statement. Specifically, the new action statement will require 
    verification of operability of the two residual heat removal (RHR) 
    trains, or initiation of power reduction with only one RHR train 
    operable, when the plant inlet water temperature is between 90 and 94 
    degrees Farenheit. The current TS requires shutdown when plant inlet 
    water temperature exceeds 90 degrees Farenheit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change does not involve any physical alteration of 
    plant systems, structures or components. The proposed change 
    provides an allowed time for the plant to continue operation with 
    plant inlet water temperature in excess of the current technical 
    specification limit of 90 degrees Fahrenheit, up to 94 degrees 
    Fahrenheit, which is less than the design limit of 95 degrees 
    Fahrenheit for plant components. The plant inlet water temperature 
    is not assumed to be an initiating condition of any accident 
    analysis evaluated in the updated safety analysis report (USAR). 
    Therefore, the allowance of a limited time for the water temperature 
    to be in excess of the current limit does not involve an increase in 
    the probability of an accident previously evaluated in the USAR. The 
    UHS [ultimate heat sink] supports operability of safety related 
    systems used to mitigate the consequences of an accident. Plant 
    operation for brief periods with plant inlet water temperature 
    greater than 90 degrees Fahrenheit up to 94 degrees Fahrenheit will 
    not adversely affect the operability of these safety-related systems 
    and will not adversely impact the ability of these systems to 
    perform their safety-related functions. Therefore, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated in the USAR.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not involve any physical alteration of 
    plant systems,
    
    [[Page 9204]]
    
    structures or components. The temperature of the plant inlet water 
    being greater than 90 degrees Fahrenheit but less than or equal to 
    94 degrees Fahrenheit for a short period does not introduce new 
    failure mechanisms for systems, structures or components not already 
    considered in the USAR. Therefore, the possibility of a new or 
    different kind of accident from any accident previously evaluated is 
    not created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change will allow an increase in plant inlet water 
    temperature above the current technical specification limit of 90 
    degrees Fahrenheit for the Ultimate Heat Sink, and delay the 
    requirement to shutdown the plant when the plant inlet water system 
    temperature limit is exceeded for 12 hours. The proposed change does 
    not alter any safety limits, limiting safety system settings, or 
    limiting conditions for operation, and the proposed temperature 
    increase will remain below the design limit cooling water input 
    value for safety-related equipment, except for the unlikely event of 
    a combination of a worst dam failure occurring with a loss of 
    coolant accident during a period of severe meteorological 
    conditions. Thus, the proposed change does not involve a significant 
    reduction in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037.
        NRC Project Director: William H. Bateman.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of application for amendment: January 22, 1999.
        Brief description of amendment: The amendment would revise 
    Technical Specification Surveillance Requirement 3.8.1.7 to better 
    match plant conditions during diesel generator (DG) testing by 
    clarifying which voltage and frequency limits are applicable during the 
    transient and steady state portions of the DG start.
        Date of publication of individual notice in Federal Register: 
    February 1, 1999 (64 FR 4902).
        Expiration date of individual notice: March 3, 1999.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, IA 52401.
    
    Illinois Power Company, Docket, No. 50-461, Clinton Power Station, 
    DeWitt County, Illinois
    
        Date of application for amendment: January 20, 1999.
        Brief description of amendment request: The proposed amendment 
    requests changes to the Technical Specification degraded voltage relay 
    setpoints.
        Date of publication of individual notice in Federal Register: 
    January 28, 1999 (64 FR 4474).
        Expiration date of individual notice: March 1, 1999.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 310 N. Quincy Street, Clinton, IL 61727.
    
    PP&L, Inc., Docket No. 50-388, Susquehanna Steam Electric Station, Unit 
    2, Luzerne County, Pennsylvania
    
        Date of amendment request: November 23, 1998.
        Brief description of amendment request: The requested changes would 
    change the allowable values for both the core spray system and the low 
    pressure coolant injection system reactor steam dome pressure-low 
    functions.
        Date of publication of individual notice in Federal Register: 
    February 1, 1999 (64 FR 4904).
        Expiration date of individual notice: March 3, 1999.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois; Docket 
    Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 1 and 
    2, Rock Island County, Illinois
    
        Date of application for amendments: November 30, 1998, as 
    supplemented by letter dated January 8, 1999.
        Brief description of amendments: The amendments relocate the 
    requirement for removal of the Reactor Protection System (RPS) shorting 
    links to the Updated Final Safety Analysis Report (UFSAR).
    
    [[Page 9205]]
    
        Date of issuance: February 8, 1999.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 170; 165 & 183; 180.
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 7, 1999. (64 FR 
    1032).
        The January 8, 1999, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
    
    Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County, 
    Michigan
    
        Date of application for amendment: March 27, 1998 (NRC-98-0033).
        Brief description of amendment: The amendment revises technical 
    specifications (TS) 3.5.2 and 3.5.3 and the associated Bases, raising 
    the minimum water level for the core spray system in the condensate 
    storage tank (CST). The amendment also removes incorrect information 
    from TS 3.5.3 regarding water inventory in the CST reserved for the 
    high pressure coolant injection and reactor core isolation cooling 
    systems.
        Date of issuance: February 8, 1999.
        Effective date: February 8, 1999, with full implementation within 
    90 days.
        Amendment No.: 131.
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 22, 1998 (63 FR 
    19967).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    Ellis Reference and Information Center, 3700 South Custer Road, Monroe, 
    Michigan 48161.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: March 25, 1998, as supplemented by 
    letter dated November 30, 1998.
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications (TSs) by modifying TS 3.9.8.1, ``Shutdown 
    Cooling and Coolant Circulation-High water Level,'' and TS 3.9.8.2, 
    ``Shutdown Coolant Circulation-Low Water Level,'' to change the minimum 
    water level above the fuel assemblies seated in the reactor vessel at 
    which the Shutdown Cooling System (SDC) is required to be maintained 
    operable, or be in operation. Also TS 3.8.1.2, ``Electric Power Systems 
    A.C. Sources Shutdown,'' and appropriate Bases are revised to make 
    wording consistent with the TS 3.9.8.1 and 3.9.8.2.
        Date of issuance: February 2, 1999.
        Effective date: This license amendment is effective as of its date 
    of issuance, to be implemented within 60 days.
        Amendment No.: 148.
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 6, 1998 (63 FR 
    25109).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 2, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit 1, Ottawa County, Ohio
    
        Date of application for amendment: October 27, 1998.
        Brief description of amendment: This amendment revises TS 3/
    4.8.2.3, ``Electrical Power Systems--DC Distribution--Operating,'' and 
    the associated bases. The surveillance requirements for battery testing 
    have been revised.
        Date of issuance: February 9, 1999.
        Effective date: February 9, 1999.
        Amendment No.: 229.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 18, 1998 (63 
    FR 64125).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, OH 43606.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio
    
        Date of application for amendment: June 30, 1998, as supplemented 
    on December 9, 1998.
        Brief description of amendment: This amendment revised Technical 
    Specification 3.1.7, ``Standby Liquid Control System,'' by increasing 
    the boron concentration in the Standby Liquid Control System for Cycle 
    8 fuel design.
        Date of issuance: February 8, 1999.
        Effective date: February 8, 1999.
        Amendment No.: 97.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 29, 1998 (63 FR 
    40562).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: October 27, 1998.
        Brief description of amendments: The amendments revised Turkey 
    Point Units 3 and 4 Technical Specifications to add the qualifications 
    for the multi-discipline supervisor.
        Date of issuance: February 3, 1999.
        Effective date: February 3, 1999.
        Amendment Nos.: 199 and 193.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 16, 1998 (63 
    FR 69341).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 3, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International
    
    [[Page 9206]]
    
    University, University Park, Miami, Florida 33199.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: July 21, 1998, as supplemented 
    October 6, December 16, and December 31, 1998.
        Brief description of amendment: The amendment changes various 
    Reactor Protection System (RPS) and Engineered Safety Feature Actuation 
    System setpoints and allowable values; corrects the specified maximum 
    reactor power level limited by the high power level RPS trip; adds a 
    new Technical Specification associated with the automatic isolation of 
    steam generator blowdown; and makes several editorial changes to 
    correct various errors and to provide needed clarification. The 
    amendment also makes changes to the applicable Bases pages and expands 
    the Bases to discuss the new requirements for the automatic isolation 
    of steam generator blowdown. However, the staff has not completed its 
    evaluation of the requested change in the trip setpoint and allowable 
    values for the steam generator water level. This portion of the request 
    will be addressed later.
        Date of issuance: February 8, 1999.
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment No.: 226.
        Facility Operating License No. DPR-65: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 12, 1998 (63 FR 
    43208).
        The October 6, December 16, and December 31, 1998, letters provided 
    clarifying information that did not change the scope of the July 21, 
    1998, application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of application for amendment: March 3, 1998, as supplemented 
    May 7, 1998.
        Brief description of amendment: The amendment revises the Millstone 
    Unit 3 licensing basis by eliminating the requirement to have the 
    recirculation spray system directly inject into the reactor coolant 
    system following a design-basis accident, with the exception of loss-
    of-coolant accident (LOCA) scenarios involving a long-term passive 
    failure. The Millstone Unit 3 licensing basis maintains the direct 
    injection requirement for scenarios, as a contingency, for situations 
    where it may be needed--as in the case of a LOCA with a long-term 
    passive failure or for beyond design-basis scenarios.
        Date of issuance: January 20, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days from the date of issuance.
        Amendment No.: 165.
        Facility Operating License No. NPF-49: Amendment revised the 
    Millstone Unit 3 licensing basis.
        Date of initial notice in Federal Register: March 25, 1998 (63 FR 
    14487).
        The May 7, 1998, letter provided clarifying information that did 
    not change the scope of the March 3, 1998, application and the initial 
    proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendment and final no 
    significant hazards consideration determination are contained in a 
    Safety Evaluation dated January 20, 1999.
        No significant hazards consideration comments received: No public 
    comments received.
        A petition to intervene was received from the Citizens Regulatory 
    Commission that was dismissed and terminated by the NRC Atomic Safety 
    Licensing Board.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: April 16, 1998.
        Brief description of amendment: The amendment changes the Technical 
    Specifications to modify a testing requirement for the emergency diesel 
    generators.
        Date of issuance: February 9, 1999.
        Effective date: February 9, 1999.
        Amendment No.: 187.
        Facility Operating License No. DPR-64: The amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 21, 1998, (63 
    FR 56256).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: June 16, 1998.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) Section 6 to relocate the Safety Review Committee 
    Reviews, Audits and Records from TS to the Quality Assurance Program 
    Section of the Final Safety Analysis Report.
        Date of issuance: February 8, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 251.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 15, 1998 (63 FR 
    38204).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: October 19, 1998.
        Brief description of amendment: This amendment eliminates 
    restrictions imposed by Technical Specification (TS) 3.0.4 for the 
    Filtration, Recirculation and Ventilation System
    
    [[Page 9207]]
    
    during fuel movement and CORE ALTERATION activities. Specifically, TS 
    Limiting Conditions for Operation 3.6.5.3.1 and 3.6.5.3.2 have been 
    revised to add a note stating that the provisions of TS 3.0.4 are not 
    applicable for initiation of handling of irradiated fuel in the 
    secondary containment and CORE ALTERATIONS provided that the plant is 
    in OPERATIONAL CONDITION 5, with reactor water level equal to or 
    greater than 22 feet 2 inches.
        Date of issuance: February 4, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 113.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 18, 1998 (63 
    FR 4121).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 4, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: September 8, 1998, as 
    supplemented December 8, 1998.
        Brief description of amendment: This amendment revised Appendix C, 
    ``Additional Conditions,'' and will allow the performance of single 
    cell charging and the use of non-Class 1E single cell battery chargers, 
    with proper electrical isolation, for charging connected cells in 
    OPERABLE Class 1E batteries. The single cell chargers will be used to 
    restore individual cell parameters to the normal limits specified in 
    Technical Specification Table 4.8.2.1-1.
        Date of issuance: February 9, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 114.
        Facility Operating License No. NPF-57: This amendment revised 
    Appendix C of the license.
        Date of initial notice in Federal Register: October 7, 1998 (63 FR 
    53954).
        The December 8, 1998, supplement provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination or expand the scope of the original Federal 
    Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: April 28, 1998, as supplemented 
    September 29, 1998, and December 8, 1998.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.4.2.1 to replace the 1% setpoint 
    tolerance limit for safety/relief valves (SRVs) with a 3% 
    setpoint tolerance limit. In addition, the amendment revises TS 4.4.2.2 
    to state that all SRVs will be re-certified to meet a 1% 
    tolerance prior to returning the valves to service after setpoint 
    testing.
        Date of issuance: February 10, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 115.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 17, 1998 (63 FR 
    33108).
        The September 29, 1998, and December 8, 1998, supplements provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination or expand the scope of 
    the original Federal Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 10, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: June 25, 1998, as supplemented 
    August 25, 1998, and December 15, 1998.
        Brief description of amendment: The amendment revised Technical 
    Specification (TS) Surveillance Requirement 4.5.1.d.2.b by deleting the 
    requirement to perform in-situ functional testing of the Automatic 
    Depressurization System safety relief valves (SRVs) during startup 
    testing activities. The amendment also revised TS Surveillance 
    Requirement 4.4.2.1 such that the 18-month channel calibration for the 
    SRV acoustic monitors will no longer require an exception to the 
    provisions of TS 4.0.4, nor adjustments to SRV full open noise levels.
        Date of issuance: February 10, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 116.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 12, 1998 (63 FR 
    43212).
        The August 25, 1998, and December 15, 1998, supplements provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination or expand the scope of 
    the original Federal Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 10, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-311, Salem Nuclear 
    Generating Station, Unit No. 2, Salem County, New Jersey
    
        Date of application for amendment: October 12, 1998.
        Brief description of amendment: This amendment allowed a one-time 
    extension of the Technical Specification (TS) surveillance interval to 
    the end of fuel Cycle 10 for certain TS surveillance requirements 
    (SRs). Specifically, the amendment extended the surveillance interval 
    in (a) SR 4.3.2.1.3 for the instrumentation response time testing of 
    each engineered safety features actuation system function, (b) SRs 
    4.8.2.3.2.f and 4.8.2.5.2.d for service testing of the 125-volt DC and 
    the 28-volt DC distribution system batteries, respectively, and (c) SR 
    4.8.2.5.2.c.2 for verification that the 125-volt DC battery connections 
    are clean, tight, and coated with anti-corrosion material. Because of 
    the length of the last outage and delays in restart, the SRs would have 
    become overdue prior to reaching the next refueling outage (2R10). The 
    SRs are to be completed during the 2R10 outage, prior to returning the 
    unit to Mode 4 (hot shutdown) upon outage completion.
        Date of issuance: February 1, 1999.
    
    [[Page 9208]]
    
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment No.: 198.
        Facility Operating License No. DPR-75: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 4, 1998 (63 FR 
    59594).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 1, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of application for amendments: November 14, 1997, as 
    supplemented by letters dated March 13, 1998, and November 10, 1998.
        Brief description of amendments: The amendments would revise the 
    licensing basis as described in Section 3.5, ``Missile Protection,'' of 
    the Updated Final Safety Analysis Report to allow the use of NUREG-
    0800, ``Standard Review Plan'' methodology in evaluating tornado-
    generated missiles.
        Date of issuance: February 9, 1999.
        Effective date: February 9, 1999, to be implemented in the next 
    periodic update of the Updated Final Safety Analysis Report (UFSAR) in 
    accordance with 10 CFR 50.71(e) that occurs after 60 days of the date 
    of issuance.
        Amendment Nos.: Unit 2--148; Unit 3--140.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the UFSAR.
        Date of initial notice in Federal Register: December 31, 1997 (62 
    FR 68315).
        The March 13, 1998, and November 10, 1998, supplemental letters 
    provided additional clarifying information and did not change the 
    original no significant hazards consideration determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated February 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
    
    Southern Nuclear Operating Company, Inc., et al. Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of application for amendments: June 26, 1998, as supplemented 
    by letters dated September 18 and November 30, 1998.
        Brief description of amendments: The amendments revise the 
    Technical Specifications (TS) as follows: (1) The Applicability of 
    Limiting Condition for Operation (LCO) 3.3.6, ``Containment Ventilation 
    Isolation Instrumentation,'' is revised to refer to TS Table 3.3.6-1; 
    the TS table is revised to add a column entitled ``Applicable Modes or 
    Other Specified Conditions.'' Then, the applicable modes for Manual 
    Initiation, Automatic Actuation Logic and Actuation Relays, and Safety 
    Injection are revised to include only Modes 1, 2, 3, and 4. Consistent 
    with this change, LCO 3.3.6, Condition C and Required Action C.2 are 
    revised to reflect that system level manual initiation and automatic 
    actuation are not required during core alterations and/or during 
    movement of irradiated fuel assemblies within containment. Appropriate 
    Bases changes are included to reflect the TS changes. (2) LCO 3.9.4 is 
    revised to allow the emergency air lock to be open during core 
    alterations and/or during movement of irradiated fuel assemblies within 
    containment. In addition, the LCO statement is revised to reflect that 
    containment ventilation isolation (CVI) would be accomplished by 
    manually closing the individual containment purge supply and exhaust 
    isolation valves as opposed to a system level manual or automatic 
    initiation, consistent with the proposed change to LCO 3.3.6. 
    Surveillance Requirement (SR) 3.9.4.2 is revised to reflect the change 
    to CVI. Appropriate Bases changes are included to reflect the TS 
    changes. (3) LCO 3.7.6 is revised to delete the words ``Redundant 
    CSTs'' from the title and LCO 3.7.6a is deleted. Appropriate Bases 
    changes are included to reflect the changes.
        Date of issuance: January 29, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: Unit 1--105; Unit 2--83.
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: October 7, 1998 (63 FR 
    53955). The supplement dated November 30, 1998, provided clarifying 
    information that did not change the scope of the application and the 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated January 29, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia.
    
    Southern Nuclear Operating Company, Inc., et al., Docket Nos. 50-424 
    and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke 
    County, Georgia
    
        Date of application for amendments: July 13, 1998, as supplemented 
    by letters dated December 16, 1998, and January 13, 1999.
        Brief description of amendments: The amendments revise Technical 
    Specification Section 1.1, Definitions, for ``Engineered Safety Feature 
    [ESF] Response Time'' and ``Reactor Trip System [RTS] Response Time'' 
    to provide for verification of response time for selected components 
    provided that the components and the methodology for verification have 
    been previously reviewed and approved by the NRC.
        Date of issuance: February 8, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: 106 and 84.
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 7, 1998 (63 FR 
    53957).
        The December 16, 1998, and January 13, 1999, letters provided 
    clarifying information that did not change the scope of the July 13, 
    1998, application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: October 29, 1998.
        Brief description of amendments: Relocates portions of Technical 
    Specification 4.8.1.1.2.g requirements regarding maintenance of the 
    diesel generator fuel oil storage tank to the Technical Requirements 
    Manual.
    
    [[Page 9209]]
    
        Date of issuance: February 8, 1999.
        Effective date: The license amendment is effective as of its date 
    of issuance, to be implemented within 30 days of issuance.
        Amendment Nos.: Unit 1--Amendment No. 102; Unit 2--Amendment No. 
    89.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 16, 1998 (63 
    FR 69347).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: November 16, 1998.
        Brief description of amendments: The amendments revise the Sequoyah 
    Nuclear Plant Technical Specification (TS) emergency diesel generator 
    surveillance requirements. The U.S. Nuclear Regulatory Commission staff 
    has found the proposed changes to be acceptable.
        Date of issuance: February 9, 1999.
        Effective date: As of the date of issuance to be implemented no 
    later than 45 days after issuance.
        Amendment Nos.: 242 and 232.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the TSs.
        Date of initial notice in Federal Register: December 2, 1998 (63 FR 
    66603).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
    
    Yankee Atomic Electric Company, Docket No. 50-29, Yankee Nuclear Power 
    Station, Franklin County, Massachusetts
    
        Date of application for amendment: August 20, 1998.
        Brief description of amendment: Revises Technical Specifications 
    (TS) through deletion of definition of SITE BOUNDARY, moves site map 
    from TS to Final Safety Analysis Report and deletion of an uneeded 
    reference to the site map.
        Date of issuance: February 3, 1999.
        Effective date: February 3, 1999.
        Amendment No.: 150.
        Possession Only License No. DPR-3: Amendment revised the Technical 
    Specifications.
        Date of initial notice in Federal Register: October 7, 1998 (63 FR 
    53962). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 3, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Greenfield Community College, 
    1 College Drive, Greenfield, Massachusetts 01301.
    
        Dated at Rockville, Maryland, this 17th day of February 1999.
    
        For the Nuclear Regulatory Commission.
    John A. Zwolinski,
    Director, Division of Licensing Project Management, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 99-4391 Filed 2-23-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
02/24/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-4391
Dates:
Immediately, to be implemented within 60 days.
Pages:
9183-9209 (27 pages)
PDF File:
99-4391.pdf