97-4573. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 38 (Wednesday, February 26, 1997)]
    [Notices]
    [Pages 8790-8807]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-4573]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from February 1, 1997, through February 13, 1997. 
    The last biweekly notice was published on February 12, 1997 (62 FR 
    6567).
    
    [[Page 8791]]
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    Involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By March 28, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public
    
    [[Page 8792]]
    
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
        Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts.
        Date of amendment request: January 30, 1997.
        Description of amendment request: The proposed amendment would 
    change the Updated Final Safety Analysis Report (FSAR) to include the 
    credit for containment overpressure in the Pilgrim Nuclear Power 
    Station net positive suction head (NPSH) analysis for the emergency 
    core cooling pumps.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Will crediting post-LOCA [loss-of-coolant accident] wetwell 
    airspace pressure in ECCS [emergency core cooling system] analyses 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated?
        Chapter 14 of the FSAR contains evaluations of the design basis 
    accidents, which include the refueling accident, the main steam line 
    break outside primary containment, the recirculation line break 
    inside primary containment, and the control rod drop accident. No 
    increase in the probability of the evaluated accidents will result 
    from crediting the post-LOCA wetwell airspace pressure because post-
    LOCA wetwell airspace pressure does not represent an accident 
    initiator but is rather a byproduct of the conditions which will 
    exist in the containment after the pipe break inside containment.
        The worst radiological consequences for the Pilgrim plant are 
    associated with the design basis LOCA which is the double guillotine 
    failure of the recirculation system piping. The radiological 
    analysis of this event, contained in FSAR Chapter 14, uses a TID-
    14844 source term and assumes a 1.5% per day leakage from the 
    containment, which is greater than the maximum leakage allowed by 
    the Technical Specifications. The results of this analysis are 
    presented in Table 14.5-2 of the FSAR and indicate substantial 
    margin when compared to 10 CFR Part 100 limits.
        The radiological consequences of the design basis accident are 
    not increased by taking credit for the post-LOCA wetwell airspace 
    pressure. Assuming containment integrity exists, the mechanism for 
    increasing the consequences of the accident would be an increased 
    leakage rate caused by an increase of the average differential 
    pressure between primary and secondary containment during the 
    accident response. However, the NPSH analyses performed for Pilgrim, 
    which credits the post-LOCA wetwell airspace, does not require that 
    the differential pressure between primary and secondary containment 
    be maintained above the minimum that exists due to the equilibrium 
    conditions based on the suppression pool temperature. Specifically, 
    the wetwell airspace pressure credited in the ECCS pump NPSH 
    analyses is provided by an increase in wetwell vapor pressure and 
    air/nitrogen partial pressure in equilibrium with increasing pool 
    temperature with an accounting for containment initial conditions 
    and leakage.
        By crediting the post-LOCA wetwell airspace pressure in the 
    calculation of NPSH, no requirement is created to purposely maintain 
    a higher containment pressure than would otherwise occur; no 
    requirement is incurred to delay operating containment heat removal 
    equipment at the highest rate possible; no requirement is incurred 
    to deliberately continue any condition of high containment pressure 
    to maintain adequate NPSH; and no requirement is incurred for the 
    purposeful addition of air/nitrogen into the containment to increase 
    the available pressure.
        Based on these reasons, the probability of accidents previously 
    evaluated is not increased, and the consequences of the design basis 
    accident are not increased.
        (2) Will crediting post-LOCA wetwell airspace pressure create 
    the possibility for new or different kinds of accidents?
        As stated above, Chapter 14 of the Pilgrim FSAR contains 
    evaluations of design basis accidents that include the refueling 
    accident, the main steam line break outside primary containment, the 
    recirculation line break inside primary containment, and the control 
    rod drop accident. New or different types of accidents are not 
    created by crediting the post-LOCA wetwell airspace pressure because 
    post-LOCA wetwell airspace pressure does not represent an accident 
    initiator but is rather a byproduct of the conditions which will 
    exist in the containment after the pipe break inside containment.
        Therefore, crediting post-LOCA wetwell airspace pressure does 
    not create the possibility for new or different kinds of accidents 
    from those previously analyzed.
        (3) Will crediting post-LOCA wetwell airspace pressure in ECCS 
    NPSH analyses involve a significant reduction in a margin of safety?
        The integrity of the primary containment and the operation of 
    the ECCS systems in combination limit the off-site doses to values 
    less than those suggested in 10 CFR 100 in the event of a break in 
    the primary system piping. In order for the ECCS pumps to meet their 
    performance requirements, the NPSH available to the pumps throughout 
    the accident response must meet their specific NPSH requirements. 
    Excess NPSH margin will not improve the performance of the ECCS 
    pumps because NPSH available must only meet NPSH requirements for 
    the pump to operate on its pump curve and meet design expectations.
        Crediting post-LOCA wetwell airspace pressure in ECCS NPSH 
    analyses increases the NPSH available to the pumps connected to the 
    suppression pool but limits the increase in NPSH available 
    consistent with the bounding leakage assumptions for the containment 
    system. The amount of post-accident pressure that is utilized in 
    ECCS NPSH analyses is calculated in a manner such that the pressure 
    credited represents a conservative lower bound of the pressure 
    available. Therefore, it is expected that the NPSH margin will 
    exceed that credited in the NPSH analyses.
        Credit for wetwell airspace pressure in NPSH analyses is not 
    required under all circumstances. If the suction strainers for the 
    ECCS pumps remain relatively free of post-LOCA debris, adequate NPSH 
    will be available without credit for the wetwell airspace pressure 
    provided by the post-LOCA heatup of the air/nitrogen gas in the 
    containment. If debris accumulates on the pump suction strainers, 
    the NPSH available to the ECCS pumps will be decreased due to the 
    head loss caused by the debris. Credit for the post-LOCA wetwell 
    airspace pressure in the analyses indicates that there is adequate 
    NPSH margin such that NPSH available will remain above NPSH 
    required, and ECCS pump performance will meet applicable 
    requirements. Based on the above discussion, credit for wetwell 
    airspace pressure in ECCS NPSH analyses does not involve a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
    
    [[Page 8793]]
    
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Patrick D. Milano, Acting.
        Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, 
    North Carolina.
        Date of amendments request: November 1, 1996.
        Description of amendments request: The amendments would revise the 
    Technical Specifications (TS) to allow full implementation of the 
    Boiling Water Reactor Owners Group (BWROG) Enhanced Option 1-A Reactor 
    Stability Long Term Solution. In Safety Evaluation Reports (SERs) 
    transmitted to Kevin P. Donovan, Chairman, BWROG, by letters from 
    Robert C. Jones, Office of Nuclear Reactor Regulation, NRC, dated June 
    21, 1996, and September 20, 1996, the NRC staff concluded that Enhanced 
    Option 1-A generic technical specifications described in Topical Report 
    NEDO-32339, Supplement 4, were acceptable for referencing in license 
    applications.
        The characteristics of a reactor system most important in 
    determining stability performance are power, core flow and power 
    distribution. The proposed changes would delete the current limits on 
    power and flow conditions in the technical specifications associated 
    with the implementation of the guidance in General Electric Service 
    Information Letter (SIL) #380, Revision 1 and the power/flow figure 
    (Figure 3.4.1.1-1), add two new specifications on the fraction of core 
    boiling boundary (FCBB) and the Period Based Detection System (PBDS) 
    and relocate certain requirements pertaining to the Average Power Range 
    Monitors (APRM) to the Core Operating Limits Report (COLR).
        The current Technical Specifications for Units 1 and 2 permit 
    single loop operation (SLO) only for a 12-hour period and there are no 
    provisions for potential alterations of safety limits or operating 
    limits because of SLO conditions. Approval of the amendment 
    applications discussed above would permit SLO operation subject to the 
    compensatory actions and requirements that address this mode of 
    operation in the revised Technical Specifications. However, Brunswick 
    Unit 2's License currently has a condition, 2.C.(5) that states that 
    the reactor shall not be made critical unless both recirculation loops 
    are in service. This License Condition also requires the plant to be 
    placed in the hot shutdown condition within 24 hours if one 
    recirculation loop becomes out-of-service. The License Condition also 
    allows one or both recirculation loops to be out-of-service for the 
    purposes of testing (not to exceed 24 hours). Whereas the License 
    Condition would permit SLO for up to 24 hours, the current TS limit SLO 
    to 12 hours. The License Condition was added to permit natural 
    circulation testing as required by the startup test program but to 
    preclude long-term SLO or operation in the natural circulation mode. 
    The startup test program was completed many years ago for Brunswick 
    Unit 2 and natural circulation operation is no longer allowed. The 
    License Condition is no longer relevant and if not deleted would negate 
    the objectives of the proposed license amendments discussed above. The 
    licensee has submitted proposed license amendments on the same date of 
    the subject application (i.e., November 1, 1996) to convert the 
    Brunswick Units 1 and 2 Technical Specifications to the Improved 
    Standard Technical Specifications (ISTS) consistent with NUREG-1433, 
    Revision 1, ``Standard Technical Specifications for General Electric 
    Plants, BWR 4.'' Attachment 6 of the later application was a proposed 
    revision of the Brunswick Unit 2 License to delete License Condition 
    2.C.(5). While the Notice of Consideration of Issuance of the ISTS 
    amendments (62 FR 3719) discussed deletion of License Condition 
    2.C.(5), the deletion is discussed in this Notice as well, since if the 
    subject amendment applications are approved, the License Condition 
    would thwart the considerable effort represented by the subject 
    amendments to finally resolve the thermal-hydraulic stability issues 
    for Brunswick Units 1 and 2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendments do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed amendments allow the implementation of the Enhanced 
    Option 1-A (E1A) long term solution to the neutronic/thermal 
    hydraulic instability issue. Current Technical Specification 
    restrictions on power and flow conditions, number of operating 
    recirculation loops and operator actions implemented to reduce the 
    probability of neutronic/thermal hydraulic instability are 
    eliminated and new stability control requirements consistent with 
    NEDO-32339, Supplement 4, are imposed. These requirements include 
    restrictions on power and flow conditions and actions associated 
    with the modified APRM flow biased scram and control rod block 
    functions. These actions include adherence to the boiling boundary 
    limit stability control prior to entry and during operation in the 
    region of the power and flow operating domain which is potentially 
    susceptible to neutronic/thermal hydraulic instability in the 
    absence of the stability control. In addition, the proposed 
    amendments require operator actions based upon a new Period Based 
    Detection System (PBDS). The PBDS is designed to provide alarm 
    indication that conditions consistent with a significant degradation 
    in the stability performance of the reactor has occurred and the 
    potential for imminent onset of neutronic/thermal hydraulic 
    instability may exist.
        The proposed amendments will permit operation in regions of the 
    power and flow operating domain postulated to be susceptible to 
    neutron/thermal hydraulic instability (i.e., Restricted and 
    Monitored Regions). Operation in these regions does not increase the 
    probability of occurrence of initiators and precursors of previously 
    analyzed accidents when neutronic/thermal hydraulic instability is 
    not possible. The proposed amendments also permit the implementation 
    of the features of the E1A solution which prevent neutronic/thermal 
    hydraulic instability including pre-emptive reactor scram upon entry 
    into the region of the power and flow operating domain most 
    susceptible to neutronic/thermal hydraulic instability (i.e., 
    Exclusion Region). Furthermore, the E1A solution requires 
    implementation of stability control prior to entry into a region of 
    the power and flow operating domain which is potentially 
    susceptible, in the absence of stability control, to neutronic/
    thermal hydraulic instability (i.e., Restricted Region). The E1A 
    solution prevents neutronic/thermal hydraulic instability during 
    operation in regions of the power and flow operating domain 
    previously excluded from operation and therefore does not 
    significantly increase the probability of a previously analyzed 
    accident.
        Operation in the regions of the power and flow operating domain 
    excluded by current Technical Specification 3/4.4.1.1 and Figure 
    3.4.1.1-1 can occur as a result of anticipated operational 
    occurrences. The severity of these transients may increase in the 
    absence of operator actions due to the potential occurrence of 
    neutronic/thermal hydraulic instability as a result of operation in 
    these regions. The proposed amendments will permit the 
    implementation of the E1A long term solution to the stability issue. 
    Required features of the E1A solution include adherence to a boiling 
    boundary limit stability control prior to selection by the operator 
    of APRM flow biased scram and control rod block function setpoints 
    which
    
    [[Page 8794]]
    
    allow operation in a region of the power and flow operating domain 
    potentially susceptible, in the absence of the stability control, to 
    neutronic/thermal hydraulic instability. Upon entry, as a result of 
    an anticipated operational occurrence, into the region most 
    susceptible to neutronic/thermal hydraulic instability during 
    operation with the boiling boundary limit stability control met, the 
    pre-emptive reactor scram prevents neutronic/thermal hydraulic 
    instability. Therefore, the consequences of an accident do not 
    significantly increase while operating with the stability control 
    met. After exiting the region requiring the stability control to be 
    met, the setpoints are automatically returned to the values 
    applicable when anticipated operational occurrences can be initiated 
    from conditions with the stability control not met. This automatic 
    actuation of the more conservative setpoints ensures that the pre-
    emptive reactor scram will prevent operation as a result of an 
    anticipated operational occurrence in the region most susceptible to 
    neutronic/thermal hydraulic instability should the operator not 
    select the more conservative setpoints appropriate for operation 
    following exit from the region requiring stability control. These 
    required features of the E1A solution prevent operation in the 
    region of the power and flow operating domain most susceptible to 
    postulated neutronic/thermal hydraulic instability by pre-emptive 
    reactor scram regardless of how the region was entered. Therefore, 
    the proposed amendments prevent the occurrence of neutronic/thermal 
    hydraulic instability as a consequence of an anticipated operational 
    occurrence and do not significantly increase the consequences of any 
    previously analyzed accident.
        2. The proposed amendments do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendments eliminate restrictions on power and flow 
    conditions and impose alternative restrictions which permit the 
    implementation of the E1A long term stability solution. The current 
    restrictions on the power and flow conditions do not prevent the 
    entry into regions of the power and flow operating domain most 
    susceptible to neutronic/thermal hydraulic instability and therefore 
    the possibility of neutronic/thermal hydraulic instability exists in 
    the absence of operator action. The required features of the E1A 
    solution implement a pre-emptive scram upon entry into the region 
    most susceptible, without operator action, to neutronic/thermal 
    hydraulic instability. The accessible operating domain allowed by 
    the proposed amendments is a subset of the power and flow operating 
    domain currently allowed. Current initiators and precursors of 
    accidents and anticipated operational occurrences can not occur with 
    new or different initial conditions. Therefore, the proposed 
    amendments do not create the possibility of a new or different kind 
    of accident from that previously evaluated.
        Concurrent with the implementation of the proposed amendments, a 
    modified Flow Control Trip Reference (FCTR) card and a new Period 
    Based Detection System (PBDS) will be installed as required by the 
    E1A solution. The function of the FCTR card is to aid the operator 
    in the identification of entry into regions of the power and flow 
    operating domain potentially susceptible to neutronic/thermal 
    hydraulic instability and to initiate a pre-emptive scram upon entry 
    into the regions most susceptible to neutronic/thermal hydraulic 
    instability. This is accomplished by altering the values of 
    setpoints of the APRM flow biased scram and the control rod block 
    functions generated by the modified FCTR card, which are existing 
    functions of the current FCTR card. The modified FCTR card design 
    includes components which may be susceptible to electromagnetic 
    interference or other environmental effects. The plant specific 
    environmental conditions (temperature, humidity, pressure, seismic, 
    and electromagnetic compatibility) have been confirmed to be 
    enveloped by the PBDS environmental qualification values and will be 
    confirmed to be enveloped by the E1A FCTR card environmental 
    qualification values prior to installation. Therefore, the potential 
    for spurious scrams or common mode failures induced by environmental 
    effects (e.g., electromagnetic interference) is considered 
    negligible. The installation of the modified FCTR card will 
    therefore not create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The function of the 
    PBDS is to provide the operator with an indication that conditions 
    consistent with a significant degradation in the stability 
    performance of the reactor has occurred and the potential for 
    imminent onset of neutronic/thermal hydraulic instability may exist. 
    This is accomplished by the installation of a new PBDS card in the 
    Neutron Monitoring System. The PBDS card takes inputs from 
    individual local power range monitors and provides displays 
    indicating alarm and status conditions to the operator in the 
    control room. These displays can not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The PBDS card design includes components which may be 
    susceptible to electromagnetic interference or other environmental 
    effects. The plant specific environmental conditions (temperature, 
    humidity, pressure, seismic, and electromagnetic compatibility) have 
    been confirmed to be enveloped by the PBDS environmental 
    qualification values and will be confirmed to be enveloped by the 
    E1A FCTR card environmental qualification values prior to 
    installation. Therefore, the installation of the PBDS card will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed amendments do not involve a significant 
    reduction in a margin of safety. The proposed amendments permit the 
    implementation of the E1A long term solution to the stability issue. 
    Under certain conditions, existing BWR designs are susceptible to 
    neutronic/thermal hydraulic instability. General Design Criterion 
    (GDC) 12 OF 10 CFR 50, Appendix A, requires thermal hydraulic 
    instability to be prevented by design or be readily and reliably 
    detected and suppressed. When the design of the reactor system does 
    not prevent the occurrence of neutronic/thermal hydraulic 
    instability, instability is an anticipated operational occurrence. 
    GDC 10 of 10 CFR 50, Appendix A, requires that specified acceptable 
    fuel design limits not be exceeded during anticipated operational 
    occurrences.
        Analyses performed by the BWROG indicate that neutronic/thermal 
    hydraulic instability induced power oscillations could result in 
    conditions exceeding the Minimum Critical Power Ratio (MCPR) Safety 
    Limit (SL) prior to detection and suppression by the current design 
    of the Neutron Monitoring System and Reactor Protection System. To 
    ensure compliance with GDC 12, the BWROG developed Interim 
    Corrective Actions (ICAs) to enhance the capability of the operator 
    to readily and reliably detect and suppress neutronic/thermal 
    hydraulic instability. The BWROG ICAs also provided additional 
    guidance for monitoring local power range monitors beyond the 
    requirements of current Technical Specification 3/4.4.1.1 to ensure 
    adequate margin to the onset of neutronic/thermal hydraulic 
    instability. Reliance on operator actions to comply with GDC 12 was 
    accepted on an interim basis by the NRC pending final implementation 
    of a long term solution to the stability issue.
        The modified design of the Reactor Protection System (APRM flow 
    biased scram) implemented with the E1A solution prevents neutron/
    thermal hydraulic instability. The E1A solution also requires 
    implementation of the stability control prior to entry into a region 
    of the power and flow operating domain which is potentially 
    susceptible, in the absence of the stability control, to neutronic/
    thermal hydraulic instability. As a result, the margin to the onset 
    of neutronic/thermal hydraulic instability provided by the existing 
    Technical Specification requirements and BWROG ICAs recommendations 
    is not significantly reduced by the implementation of the E1A 
    solution. The E1A solution assures compliance with GDC 12 by the 
    prevention of neutronic/thermal hydraulic instability and therefore 
    precludes neutronic/thermal hydraulic instability from becoming a 
    credible consequence of an anticipated operational occurrence. The 
    consequences of anticipated operational occurrences and the margin 
    to the MCPR SL will not change upon the implementation of the E1A 
    solution. Therefore, the proposed amendments do not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    [[Page 8795]]
    
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart (Acting).
        Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois.
        Date of amendment request: January 20, 1997.
        Description of amendment request: The proposed amendments would 
    relocate the surveillance requirements for selected instrumentation 
    from the Technical Specifications to licensee controlled documents 
    because the instrumentation provides indication or an alarm only. The 
    affected surveillance requirements are: 4.1.3.5.b, ``Control Rod Scram 
    Accumulators''; 4.5.1.d.2.c, `` Emergency Core Cooling Systems--
    Operating''; 4.5.3.1.b, ``ECCS--Suppression Chamber''; and 4.6.2.1.c, 
    ``Containment Systems--Suppression Chamber''. In addition, the proposed 
    amendments would replace TS SR 4.4.3.2.1, ``Reactor Coolant System 
    Leakage'' and SR 4.5.1.d.1, ``ECCS--Operating'' with surveillances more 
    appropriate to the associated LCOs and action statements. Also, the 
    proposed amendments add an action statement to TS 3.5.1, ``ECCS--
    Operating'' regarding pressure of the ADS accumulator backup compressed 
    gas system bottle, and delete action statements 3.5.3.c, 3.5.3.d, 
    3.6.2.1.c and 3.6.2.1.d regarding suppression chamber water level 
    instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        The proposed change relocates instrumentation requirements, 
    which provide no post-accident function from the Technical 
    Specifications to the Bases, UFSAR, procedures, or other plant 
    controlled documents. These requirements are part of routine 
    operational monitoring and are not considered in the safety 
    analysis. The Bases, UFSAR, procedures, and other plant controlled 
    documents containing the relocated information will be maintained in 
    accordance with 10 CFR 50.59. In addition to 10 CFR 50.59 
    provisions, the Technical Specification Bases are subject to the 
    change control provisions in the Administrative Controls Chapter of 
    the Technical Specifications. The UFSAR is subject to the change 
    control provisions of 10 CFR 50.71(e), and plant procedures and 
    other plant controlled documents are subject to controls imposed by 
    plant administrative procedures, which endorse applicable 
    regulations and standards. Since any changes to the Bases, UFSAR, 
    procedures, or other plant controlled documents will be evaluated 
    per the requirements of 10 CFR 50.59, no significant increase in the 
    probability or consequences of an accident previously evaluated will 
    be allowed. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The Reactor Coolant Operational Leakage limits monitoring 
    surveillance 4.4.3.2.1 has been modified to eliminate procedural 
    details of what instrumentation/leakage detection systems to use in 
    verifying limits. The proposed surveillance requires verification 
    that the reactor coolant system leakage is within limits at the same 
    frequency as the current surveillance requirement. The reactor 
    coolant leakage detection systems operability requirements are 
    controlled by Technical Specification 3/4.4.3.1. Since any changes 
    to procedures describing the method of monitoring leakage will be 
    evaluated per the requirements of 10 CFR 50.59, no significant 
    increase in the probability or consequences of an accident 
    previously evaluated will be allowed. Therefore, this change does 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The monitoring action and the surveillance requirements added 
    for the Automatic Depressurization System (ADS) pneumatic supply 
    help assure the continued operability of ADS for the mitigation of 
    accidents involving high reactor vessel pressure and the loss of the 
    high pressure core spray system. The surveillance frequency is 
    reasonable for the ADS supply header pressure due to the redundancy 
    of the instrument nitrogen system, [and] several alarms [that warn] 
    of system trouble. The ADS accumulator backup compressed gas system 
    bottle pressure monitoring surveillance frequency and the proposed 
    action on low bottle pressure is reasonable due to the [presence of 
    the] ADS accumulator check valves and the [availability of the] 
    normal ADS supply header. Therefore, this change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        The proposed change does not involve a physical alteration of 
    the plant (no new or different type of equipment will be installed) 
    or a change in the methods governing normal plant operation. The 
    proposed change will not impose or eliminate any requirements, and 
    adequate control of the requirements will be maintained. Thus, these 
    changes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Involve a significant reduction in the margin of safety 
    because:
        The proposed change will not reduce a margin of safety because 
    it has no impact on any safety analysis assumption. In addition, the 
    requirements to be transposed from the Technical Specifications to 
    procedures, or other plant controlled documents are the same as the 
    existing Technical Specifications. Since any future changes to these 
    requirements in the Bases, UFSAR, procedures, or other plant 
    controlled documents will be evaluated per the requirements of 10 
    CFR 50.59, no significant reduction in a margin of safety will be 
    allowed.
        Based on 10 CFR 50.92, the existing requirement for NRC review 
    and approval of revisions to these requirements proposed for 
    relocation does not have a specific margin of safety upon which to 
    evaluate. However, since the proposed change is consistent with the 
    BWR Standard Technical Specifications, NUREG-1434, approved by the 
    NRC Staff, revising the Technical Specifications to reflect the 
    approved level of instrumentation requirements ensures no 
    significant reduction in the margin of safety.
        The Reactor Coolant Operational Leakage limits monitoring 
    surveillance 4.4.3.2.1 has been modified to eliminate procedural 
    details of what instrumentation/leakage detection systems to use in 
    verifying limits. The proposed surveillance requires verification 
    that the reactor coolant system leakage is within limits at the same 
    frequency as the current surveillance requirement. The reactor 
    coolant leakage detection systems operability requirements are 
    controlled by Technical Specification 3/4.4.3.1. Because there are 
    no changes to either the reactor coolant leakage detection systems 
    and the reactor coolant leakage continues to be maintained within 
    the specified limits, at the required frequency, there is no 
    reduction in the margin of safety.
        The monitoring action and the surveillance requirements added 
    for the Automatic Depressurization System (ADS) pneumatic supply 
    help assure the continued operability of ADS for the mitigation of 
    accidents involving high reactor vessel pressure and the loss of the 
    high pressure core spray system. This helps assure ADS is maintained 
    in a ready status. The previous TS SRs only tested the 
    instrumentation, and did not verify the parameter remained within 
    limits. Therefore, the margin of safety is not reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
        Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan.
    
    [[Page 8796]]
    
        Date of amendment request: January 10, 1996.
        Description of amendment request: The proposed amendment would 
    revise test requirements for the containment emergency escape airlock.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The following evaluation supports the finding that operation of 
    the facility in accordance with the proposed change to the Technical 
    Specifications would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change does not alter any plant operating 
    conditions, operating practices, equipment design, equipment 
    settings, or equipment capabilities. Therefore, operation of the 
    facility in accordance with the proposed change will not involve an 
    increase in the probability of an accident. This determination is 
    made because the full pressure test and the seal contact check 
    provides reasonable assurance that the Emergency Escape Airlock 
    doors will act as designed to maintain containment integrity. 
    Procedures are established to test seal integrity with full pressure 
    airlock test and to verify the seal contact following the test. 
    Acceptance criteria are established for each evolution. Failure to 
    meet the acceptance criteria would result in corrective action to 
    restore the Emergency Escape Airlock to the intended condition.
        The proposed change defines the pressure tests required for the 
    Emergency Escape Airlock and specifies the method used to restore 
    the airlock door seals after full pressure testing. Due to the 
    design of the airlock, the doors must be opened after testing. This 
    change recognizes the practice of verifying the final integrity of 
    the airlock by verifying door seal contact. Since the pressure test 
    does not load the door seals in the same direction as a design basis 
    accident, this seal contact check provides better assurance that the 
    door is sealed than alternative pressure tests. The Emergency Escape 
    Airlock continues to be capable of performing its design function 
    and the consequences of those accidents previously evaluated will 
    not increase.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed change does not alter any plant operating 
    conditions, operating practices, equipment design, equipment 
    settings, or equipment capabilities. Therefore, operation of the 
    facility in accordance with the proposed change will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change requires testing of the Emergency Escape 
    Airlock at full pressure (greater than or equal to Pa) rather 
    than a reduced pressure between-the-seals test. This reduced 
    pressure test is allowed by the existing Technical Specifications 
    when the door is opened during periods when containment integrity is 
    required. The door seal contact check and restoration will provide 
    assurance that the Emergency Escape Airlock is capable of performing 
    its design function after the doors are opened during recovery from 
    full pressure testing. Implementation of these test requirements and 
    meeting the acceptance criteria will ensure that containment 
    integrity with respect to the Emergency Escape Airlock will be 
    maintained. Therefore, there will be no reduction in the margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: John N. Hannon.
        Duke Power Company, Docket Nos. 50-269, 270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina.
        Date of amendment request: February 5, 1997 (TSC 96-11)
        Description of amendment request: The proposed changes would 
    reflect replacement of the existing nuclear instrumentation with an 
    enhanced wide range nuclear instrumentation system that provides more 
    channels and continuous coverage from the source to above the power 
    range. As a result: (1) The various references to Intermediate Range of 
    nuclear instrumentation would be eliminated and replaced with reference 
    to Wide Range instrumentation; (2) the minimum number of operable 
    Source and Wide Range Nuclear Instrumentation channels that are 
    available and that are required to be operable in Table 3.5.1-1 would 
    be increased; (3) the minimum power level specified in Note (c) of 
    Table 3.5.1-1 would be changed from 10-10 amps on the intermediate 
    range instrument channels to 4 x 10-4% rated power on the wide 
    range instrument channels; and (4) entries that specify the Wide Range 
    Nuclear Instrumentation, the number of Required Operable Channels, 
    reference to a new Action Statement, and Applicability would be added 
    to Table 3.5.6-1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Will the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No. The proposed amendment to the Oconee Technical 
    Specifications is associated with the implementation of an enhanced 
    nuclear instrumentation system. The new Gamma Metrics system 
    provides twice the number of channels of neutron detectors for use 
    during both normal plant operations and post-accident monitoring. 
    The proposed change will make Oconee's Technical Specifications 
    consistent with a nuclear instrumentation system that meets the 
    reliability and redundancy requirements of Regulatory Guide 1.97. 
    Additionally, the new Technical Specifications will be more 
    conservative in terms of stating the minimum number of operable 
    channels required, since there are now a greater number of redundant 
    channels available. Assuring that the nuclear instrumentation at 
    Oconee is more reliable and more redundant, does not affect the 
    probability of an occurrence of an accident, since this system is a 
    monitoring system and not an accident initiator. However, these 
    characteristics (increased reliability and redundancy) could provide 
    additional capability to deal with the consequences of post-accident 
    situations.
        (2) Will the change create the possibility of a new or different 
    kind of accident from any [kind of accident] previously evaluated?
        No. The proposed amendment to Oconee Technical Specifications 
    involves the implementation of an enhanced nuclear instrumentation 
    system. By implementing a nuclear instrumentation system that meets 
    the provisions of Regulatory Guide 1.97, Oconee's ability for 
    neutron monitoring is enhanced during normal operations and post-
    accident recovery. The Source Range nuclear instrumentation system 
    is utilized for monitoring purposes only, while the Wide Range 
    provides a control rod withdrawal interlock based on high startup 
    rate. The new Gamma Metrics detectors have been shown to be more 
    reliable, accurate, and redundant than Oconee's original detectors. 
    Therefore, changing the Oconee Technical Specifications to be 
    consistent with the current nuclear instrumentation arrangement, as 
    proposed in this amendment request, has no effect on the possibility 
    of any type of accident: new, different, or previously evaluated.
        (3) Will the change involve a significant reduction in a margin 
    of safety?
        No. Margin of safety is associated with confidence in the 
    ability to maintain the fission product barriers (i.e., fuel and 
    fuel cladding, Reactor Coolant System pressure boundary, and 
    containment structure) to limit the level of radiation dose to the 
    public. The proposed Technical Specifications amendment will 
    establish operability requirements for an enhanced nuclear 
    instrumentation system at Oconee. By
    
    [[Page 8797]]
    
    implementing a more reliable and redundant nuclear instrumentation 
    system, Oconee's post-accident monitoring capability is enhanced. 
    Therefore, the ability to protect the public from radiation dose is 
    further assured, and no reduction in any existing margin of safety 
    will occur.
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691.
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036.
        NRC Project Director: Herbert N. Berkow.
        Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi.
        Date of amendment request: October 22, 1996.
        Description of amendment request: The proposed amendment would 
    revise Figure 3.4.11-1, ``Minimum Reactor Vessel Metal Temperature vs. 
    Reactor Vessel Pressure,'' in Limiting Condition for Operation 3.4.11, 
    ``RCS [Reactor Coolant System] Pressure and Temperature (P/T) Limits,'' 
    of the Technical Specifications (TSs). The existing curve is valid only 
    up to 10 Effective Full Power Years (EFPYs) and would be revised to be 
    valid up to 32 EFPYs.
        The proposed curves, pages 1 through 5 of Figure 3.4.11-1, have 
    been drawn for five different EFPY periods: 16, 20, 24, 28 and 32. 
    There are two sets of curves attached to the licensee's application. 
    The first set of curves (Attachment 3) would replace the existing curve 
    in TS Figure 3.4.11-1. The second set of curves (Attachment 4) are 
    duplicates of the Attachment 3 curves except that these curves also 
    contain detailed information used in development of the curves and 
    would be included in the next update of the Updated Final Safety 
    Analysis Report (UFSAR) for information.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, in its application for the proposed amendment, which is 
    presented below:
    
        (A) The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        Regulatory Guide 1.99, Revision 2 is currently used to prepare 
    the pressure-temperature limit curves and is inherently conservative 
    for Boiling Water Reactors (BWRs). [Grand Gulf Unit 1 is a BWR.] The 
    proposed Technical Specification Figure 3.4.11-1 was prepared in 
    accordance with the requirements of 10CFR50 [10 CFR Part 50], 
    Appendix G [(Fracture Toughness Requirements)], and using NRC 
    approved methodology outlined in NRC Regulatory Guide 1.99, Revision 
    2, ``Radiation Embrittlement of Reactor Vessel Materials.'' 
    Operation of the plant within the limitations of the proposed figure 
    will ensure that the Requirements of 10CFR50 [10 CFR Part 50], 
    Appendix G are met up to and including 32 Effective Full Power Years 
    (EFPY) of operation. The proposed changes assure that the existing 
    safety limits are not exceeded due to changing Reactor Vessel 
    conditions by continued incorporation of the effect of neutron 
    radiation embrittlement of vessel materials into the proposed 
    curves.
        The curves have also been editorially enhanced by removal of 
    phrases used for validation of the curves. Having the phrases on the 
    TS (Technical Specification) curves distracts from the intended 
    purpose which is to maintain operation of the reactor to the right 
    of the curves. Operators, in performance of their job function, do 
    not need this information to comply with TS Limiting Condition for 
    Operation (LCO) 3.4.11. This change also revises the curve labeling 
    consistent with the terminology used in Table 1 of 10CFR50 [10 CFR 
    Part 50], Appendix G. These enhancements and revisions have no 
    impact on the operation of the plant since they are editorial in 
    nature and do not change the technical content of the curves.
        Therefore, the proposed change does not significantly increase 
    the probability or consequences of an accident previously evaluated.
        (B) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The pressure-temperature curves are controlled by the Technical 
    Specifications and are determined using the conservative methodology 
    in NRC Regulatory Guide 1.99, Revision 2, ``Radiation Embrittlement 
    of Reactor Vessel Materials.'' The proposed pressure-temperature 
    limit curves are inherently conservative, therefore, the possibility 
    of failure of the reactor vessel is not increased. The proposed 
    curves establish new periods of applicability (16, 20, 24, 28, and 
    32 EFPY) for the current pressure-temperature limitations based on 
    NRC methodology in Regulatory Guide 1.99 and actual fluence 
    measurements. These limitations are appropriate up to and including 
    32 EFPY exposure and operation of the plant within the figure's 
    limitations will ensure that the requirements of 10CFR50 [10 CFR 
    Part 50], Appendix G are met for that time frame. No physical plant 
    modifications or new operating configurations result from these 
    changes. These changes do not adversely affect the design or 
    operation of any system or component important to safety, rather 
    they establish limits to assure that operations remain within 
    acceptable safety boundaries.
        The curves have also been editorially enhanced by removal of 
    phrases used for validation of the curves. Having the phrases on the 
    TS curves distracts from the intended purpose which is to maintain 
    operation of the reactor to the right of the curves. Operators, in 
    performance of their job function, do not need this information to 
    comply with TS Limiting Condition for Operation (LCO) 3.4.11. This 
    change also revises the curve labeling consistent with the 
    terminology used in Table 1 of 10CFR50 [10 CFR Part 50], Appendix G. 
    These enhancements and revisions have no impact on the operation of 
    the plant since they are editorial in nature and do not change the 
    technical content of the curves.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        (C) The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed curves were developed using the methodology of 
    Regulatory Guide 1.99, Revision 2, ``Radiation Embrittlement of 
    Reactor Vessel Materials.'' This methodology includes an allowance 
    for margin that is to be included in the upper-bound values of the 
    adjusted reference temperature (ART). The proposed changes maintain 
    the existing margins of safety by modifying the operating limits 
    based on the most limiting of the actual reference temperature 
    shifts. These new limits consider the most limiting pressure vessel 
    material. The revised analysis demonstrates that the existing 
    Technical Specification [TS] pressure-temperature limit curves are 
    applicable for periods of 16, 20, 24, 28, and 32 EFPY. Using the 
    methodology in NRC Regulatory Guide 1.99 Revision 2 and fluence 
    based on actual exposure provides for additional conservatism, and 
    therefore [,] further assures the existence of current margins of 
    safety. The proposed pressure-temperature limit curves are 
    inherently conservative and provide sufficient margin to ensure the 
    integrity of the reactor vessel.
        The curves have also been editorially enhanced by removal of 
    phrases used for validation of the curves. Having the phrases on the 
    TS curves distracts from the intended purpose which is to maintain 
    operation of the reactor to the right of the curves. Operators, in 
    performance of their job function, do not need this information to 
    comply with TS Limiting Condition for Operation (LCO) 3.4.11. This 
    change also revises the curve labeling consistent with the 
    terminology used in Table 1 of 10CFR50 [10 CFR Part 50], Appendix G. 
    These enhancements and revisions have no impact on the operation of 
    the plant since they are editorial in nature and do not change the 
    technical content of the curves.
        Continuing commitment to the methodology contained in NRC 
    Regulatory Guide 1.99, Rev. 2, will ensure that the most limiting 
    plate or beltline weld material will be utilized in the 
    determination of the pressure-temperature limits for any future 
    curve changes.
    
    [[Page 8798]]
    
        Therefore, the proposed change does not result in a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, NW., 12th Floor, Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
        Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana.
        Date of amendment request: January 10, 1997.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TSs) for reactor pressure vessel 
    pressure and temperature (P-T) limits to replace the curves for 2 
    effective full power years (EFPY) with curves for 12 EFPY. The P-T 
    curves are used for heatup, cooldown, and inservice leak and 
    hydrostatic testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Pressure-temperature (P-T) limits (RBS Technical Specifications 
    Figure 3.4.11-1) are imposed on the reactor coolant system to ensure 
    that adequate safety margins against nonductile or rapidly 
    propagating failure exist during normal operation, anticipated 
    operational occurrences, and system hydrostatic tests. The P-T 
    limits are related to the nil-ductility reference temperature, 
    RTNDT, as described in ASME Section III, Appendix G. Changes in 
    the fracture toughness properties of [Reactor Pressure Vessel] RPV 
    beltline materials, resulting from the neutron irradiation and the 
    thermal environment, are monitored by a surveillance program in 
    compliance with the requirements of 10 CFR [Part] 50, Appendix H. 
    The effect of neutron fluence on the nil-ductility reference 
    temperature of pressure vessel steel is predicted by methods given 
    in Regulatory Guide [RG] 1.99, Rev. 2.
        The revised P-T limits of this amendment request were 
    established based on adjusted reference temperatures developed in 
    accordance with the procedures prescribed in Reg. Guide [RG] 1.99, 
    Rev. 2, Regulatory Position C.1. Calculation of adjusted reference 
    temperature by these procedures includes a margin term to ensure 
    conservative, upper-bound values are used for the calculation of the 
    P-T limits. Stress intensity factors used to compute the pressures 
    were calculated in accordance with, and include the required safety 
    factors given in ASME Section III, Appendix G. The limits 
    established by the lower portion of the P-T curves, which cover the 
    discontinuity (non-beltline) regions of the vessel (e.g., flanges, 
    nozzles, etc.), were retained throughout this current analysis. The 
    limits established by the lower portion of these curves do not 
    change as they are not affected significantly by the neutron 
    fluence.
        This change is not related to any accidents previously 
    evaluated. The proposed change will provide for approved P-T limit 
    curves which are valid through 12 EFPY. This change will not affect 
    any Safety Limits, Power Distribution Limits, or Limiting Conditions 
    for Operation. The proposed change will not affect reactor pressure 
    vessel [RPV] performance as no physical changes are involved and RBS 
    vessel P-T limits will remain conservative in accordance with Reg. 
    Guide [RG] 1.99, Rev. 2 and ASME Section III, Appendix G 
    requirements. The proposed change will not cause the reactor 
    pressure vessel [RPV] or interfacing systems to be operated outside 
    of their design or testing limits. Also, the proposed change will 
    not alter any assumptions previously made in evaluating the 
    radiological consequences of accidents. The proposed change ensures 
    that adequate margins against brittle fracture of the vessel are 
    maintained through 12 EFPY of reactor operations. Therefore, the 
    probability or consequences of accidents previously evaluated will 
    not be increased by the proposed change.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change is a revision of Technical Specification 
    Figure 3.4.11-1 to show P-T limit curves valid through 12 EFPY. The 
    revised P-T limits have been established in accordance with 
    applicable NRC regulations and the ASME Code. This proposed change 
    does not involve a modification of the design of plant structures, 
    systems, or components. The proposed change will not impact the 
    manner in which the plant is operated as plant operating and testing 
    procedures will not be affected by the change. The proposed change 
    will not degrade the reliability of structures, systems, or 
    components important to safety (ITS) as equipment protection 
    features will not be deleted or modified, equipment redundancy or 
    independence will not be reduced, supporting system performance will 
    not be downgraded, the frequency of operation of ITS equipment will 
    not be imposed. No new accident types or failure modes will be 
    introduced as a result of the proposed change. Therefore, the 
    proposed change does not create the possibility of a new or 
    different kind of accident from that previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        As stated in the River Bend SER, ``Appendices G and H of 10 CFR 
    50 describe the conditions that require pressure-temperature [P-T] 
    limits and provide the general bases for these limits. These 
    appendices specifically require that pressure-temperature [P-T] 
    limits must provide safety margins at least as great as those 
    recommended in the ASME Code, Section III, Appendix G. * * * Until 
    the results from the reactor vessel surveillance program become 
    available, the staff will use RG 1.99, Revision 1 [now Revision 2] 
    to predict the amount of neutron irradiation damage. * * * The use 
    of operating limits based on these criteria--as defined by 
    applicable regulations, codes, and standards--will provide 
    reasonable assurance that nonductile or rapidly propagating failure 
    will not occur, and will constitute an acceptable basis for 
    satisfying the applicable requirements of GDC 31.''
        Bases for RBS Technical Specification 3.4.11 states: ``The P/T 
    [P-T] limits are not derived from Design Basis Accident (DBA) 
    analyses. They are prescribed during normal operation to avoid 
    encountering pressure, temperature, and temperature rate of change 
    conditions that might cause undetected flaws to propagate and cause 
    nonductile failure of the RCPB, a condition that is unanalyzed. * * 
    * Since the P/T [P-T] limits are not derived from any DBA, there are 
    no acceptance limits related to the P/T [P-T] limits. Rather, the P/
    T [P-T] limits are acceptance limits themselves since they preclude 
    operation in an unanalyzed condition.''
        This amendment request proposes P-T limit curves which will be 
    valid through 12 EFPY. The proposed P-T limits were established 
    based on adjusted reference temperatures for vessel beltline 
    material calculated in accordance with Regulatory Position 1 of Reg. 
    Guide [RG] 1.99, Rev. 2 and pressures calculated in accordance with 
    ASME Section III, Appendix G requirements. Required margins and 
    safety factors were included to ensure that conservative, upper-
    bound values were used in calculation of the P-T limits. The 
    proposed change will not affect any Safety Limits, Power 
    Distribution Limits, or Limiting Conditions for Operation. The 
    proposed change does not represent a change in initial conditions, 
    or in a system response time, or in any other parameter affecting 
    the course of an accident analysis supporting the Bases of any 
    Technical Specification. The proposed P-T limits provide adequate 
    safety margins against brittle failure of the reactor vessel through 
    12 EFPY of power operations. For these reasons, the proposed changes 
    do not involve a reduction in any margins of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
    [[Page 8799]]
    
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803.
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, NW., Washington, DC 20005.
        NRC Project Director: William D. Beckner.
        Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana.
        Date of amendment request: January 20, 1997.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TSs) to allow the use of flow 
    control spectral shift strategies to increase cycle energy; an 
    estimated additional 30 days at full power. The request is based on a 
    General Electric (GE) Maximum Extended Load Line Limit (MELLL) analysis 
    for the River Bend Station.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not significantly increase the 
    probability or consequences of an accident previously evaluated.
        Abnormal operational transients or accidents analyzed in the SAR 
    have been examined for any impact caused by MELLL operation. The 
    limiting abnormal operation transients, including the Generator Load 
    Rejection with No Bypass (LRNBP) event and the Feedwater Controller 
    Failure (FWCF) maximum demand event, have been evaluated in detail. 
    The LOCA [Loss-of-Coolant Accident], Fuel Loading Error (FLE), rod 
    drop accident, rod withdrawal error, and the Anticipated Transient 
    Without Scram (ATWS) analyses have also been evaluated for the 
    effects of MELLL operation. The flow and power dependent [Minimum 
    Critical Power Ratio] MCPR curves for off-rated and rated conditions 
    and the [Maximum Average Planar Linear Heat Generation Rate] MAPLHGR 
    criteria establish limits on power operation. These limits ensure 
    that the core is operated within the assumptions and initial 
    conditions of the transient or accident analyses. Operation within 
    these limits will ensure that the consequences of a transient or 
    accident remain within the acceptable limits of the analyses.
        The [Average Power Range Monitor] APRM scram in the Technical 
    Specifications [TSs] and affected rod block setpoints are revised to 
    ensure that operation remains within the analyzed MELLL region. This 
    restriction ensures the consequences of abnormal operation and 
    accidents are acceptable. The probability of an accident is not 
    affected by the proposed Technical Specification [TS] changes since 
    no systems or equipment which could initiate an accident are 
    affected. Therefore, the proposed changes do not significantly 
    increase the probability or consequences of any previously evaluated 
    accident.
        2. The request does not create the possibility of occurrence of 
    a new or different kind of accident from any accident previously 
    evaluated.
        Operation in the MELLL domain expands the current power/flow 
    along the 121% rod line to 100% power at 75% rated core flow and 
    improves flexibility and capacity factor. Abnormal operation 
    transients or accidents have been evaluated and the most limiting 
    cases have been analyzed for applicability for operation in the 
    MELLL region. The proposed Technical Specification [TS] changes 
    prohibit power operation outside the MELLL region and do not 
    constitute or require any system or equipment changes that might 
    create an accident of a different type then previously evaluated. 
    The MAPLHGR, the power and flow dependent MCPR and [Liner Heat 
    Generation Rate] LHGR and the revised Technical Specifications [TSs] 
    will continue to assure that plant operation is consistent with the 
    assumptions, initial conditions and assumed power distribution and 
    therefore will not create a new type of accident. The proposed 
    Technical Specification [TS] changes do not introduce any new modes 
    of plant operation nor involve new system interactions. Therefore, 
    the proposed changes do not create the possibility of a new or 
    different kind of accident from any previous analyzed.
        3. The request does not involve a significant reduction in a 
    margin of safety.
        The proposed Technical Specifications [TSs] prohibit power 
    operation outside the allowable MELLL region. The transients and 
    accidents described in the SAR are evaluated for operation in the 
    MELLL region. NEDC-32611, ``MELLL Analysis for River Bend Station 
    Reload 6 Cycle 7,'' shows that the OLMCPR for operation in the MELLL 
    region is bounded by the OLMCPR established for current conditions 
    (100% power/107% flow). The thermal limits MCPR and LHGR curves and 
    the MAPLHGR limits establish limits on power operation and thereby 
    ensure that the core is operated within the assumptions and initial 
    conditions of the transient and accident analyses.
        As demonstrated in the analysis provided in Attachment 4, [the 
    proposed amendment request] operation within these limits, using the 
    MCPR limits, LHGH limits and MAPLHGR criteria, will ensure that the 
    margin of safety will be maintained to the same level described in 
    the Technical Specifications Bases and the SAR and the consequences 
    of the postulated transient or accidents are not increased. The MCPR 
    safety limit, mechanical performance limits and overpressure limit 
    are not exceeded during any transient or postulated accident. 
    Therefore, the proposed Technical Specifications [TSs] to allow 
    operation in the MELLL region do not involve a significant reduction 
    in margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803.
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005.
        NRC Project Director: William D. Beckner.
    
        Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine.
        Date of amendment request: February 7, 1997.
        Description of amendment request: The proposed amendment would 
    modify Technical Specification 3.12 to require both 115 kV incoming 
    lines to be operable when the reactor is critical; allow continued 
    operations for up to 72 hours with one 115 kV incoming line inoperable; 
    allow continued operations for up to 24 hours with both 115 kV incoming 
    lines inoperable; apply the increased operability requirements 
    described above to another affected remedial action; incorporate minor 
    editorial changes to uniformly apply the usage of the term 
    ``operable;'' and change the basis section to be consistent with the 
    proposed changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes to Specification 3.12.B do not involve a 
    physical change to the plant or the maintenance of the plant. The 
    proposed changes increase the operating requirements associated with 
    the operability of the 115 kV incoming lines beyond that currently 
    required by Technical Specifications. For those accidents previously 
    evaluated, the more restrictive operability requirements associated 
    with maintaining both 115 kV incoming lines operable and the more 
    restrictive remedial action times result in increased assurance that 
    station service power will be available when required. This 
    increased availability will be achieved because elective maintenance 
    on the offsite power system will be significantly restricted and the 
    restoration of inoperable 115 kV incoming lines will be treated with 
    greater urgency. The increased
    
    [[Page 8800]]
    
    assurance of availability will result in a decrease in the 
    probability or consequences of these postulated accidents.
        However, the more restrictive remedial action times decrease the 
    restoration period and consequently increase the possibility that 
    successful restoration may not be achieved, given an outage of the 
    115 kV power system. A unit shutdown without offsite power would 
    then be commenced. This evolution would involve a unit shutdown 
    without the availability of equipment such as the reactor coolant 
    pumps, condensate pumps and main feedwater pumps. Although none of 
    these components are credited as available for the mitigation of the 
    consequences of accidents previously evaluated, the probability of 
    the occurrence of certain accidents is increased without them.
        Although the combination of these considerations could involve 
    an increase in the probability of accidents previously evaluated, 
    the increase would not be significant due to the low probability of 
    independent failures or common cause failures of both of the 115 kV 
    incoming lines. There is no increase in the consequences of any 
    accident previously evaluated as a result of these proposed 
    Technical Specification changes. The proposed Technical 
    Specification changes are consistent with the Standard Technical 
    Specifications approved by the NRC. The proposed changes, therefore, 
    will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed Technical Specification change does not involve a 
    change to the physical plant or to the physical configuration of the 
    offsite power system. The effect of the proposed change will be to 
    increase the availability of the offsite power system when required. 
    In addition, the proposed change will increase the possibility of a 
    unit shutdown without offsite power operable. However, the accidents 
    previously evaluated assume a simultaneous loss of offsite power, 
    design basis accident and worst case single failure as part of the 
    design basis. The proposed changes do not result in the creation of 
    a unique operating condition or a configuration that has not been 
    previously evaluated. Therefore, the proposed change does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        This proposed change modifies Technical Specification 3.12 to be 
    consistent with the Standard Technical Specifications. The proposed 
    Technical Specification change maintains the current margin of 
    safety which is based upon supplying power to engineered safeguards. 
    Adequate sources of power remain available for the operation of the 
    engineered safeguards equipment. Therefore, the proposed change 
    would not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578.
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011.
        NRC Project Director: Patrick D. Milano, Acting.
    
        Northeast Nuclear Energy Company, et al., Docket Nos. 50-245, 50-
    336, and 50-423, Millstone Nuclear Power Station, Unit Nos. 1, 2, and 
    3, New London, Connecticut.
        Date of amendment request: February 3, 1997.
        Description of amendment request: The licensee has proposed to 
    revise Section 6, ``Administrative Controls,'' of the Millstone Unit 
    Nos. 1, 2, and 3 Technical Specifications to reflect organizational 
    changes that have been implemented in the Nuclear Division.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    * * * The proposed changes do not involve a [significant hazards 
    consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        No design basis accidents are affected by these proposed 
    changes. The proposed changes are administrative in nature and are 
    being proposed to reflect the organizational changes which become 
    effective on February 3, 1997. The unit level responsibilities of 
    the Executive Vice President--Nuclear are assigned to the Officers 
    for the individual Millstone units. The site level responsibilities 
    of the Executive Vice President--Nuclear are shared by the Senior 
    Vice President and CNO [Chief Nuclear Officer]--Millstone and the 
    President and Chief Executive Officer. The changes to the SORC [Site 
    Operations Review Committee] and the three unit[s'] PORC [Plant 
    Operations Review Committee] reflect changes in job function or job 
    position titles only.
        No safety systems are adversely affected by the proposed 
    changes, and no failure modes are associated with the changes.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        Because there are no changes in the way plants are operated due 
    to this administrative change, the potential for an unanalyzed 
    accident is not created. There is no impact on plant response, and 
    no new failure modes are introduced. These proposed administrative 
    and editorial changes have no impact on safety limits or design 
    basis accidents, and they have no potential to create a new or 
    unanalyzed event. The changes to the SORC and the three unit[s'] 
    PORC reflect changes in job function or job position titles only.
        3. Involve a significant reduction in a margin of safety.
        The changes do not directly affect any protective boundaries nor 
    do they impact the safety limits for the protective boundaries. 
    These proposed changes are administrative and editorial in nature. 
    Therefore, there is no reduction in the margin of safety. These 
    changes do not reduce the margin of safety provided by the PORC and 
    the SORC review and approval of changes to the operations of the 
    Millstone Unit Nos. 1, 2, and 3.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
        Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut.
        Date of amendment request: February 5, 1996.
        Description of amendment request: The amendment would delete a 
    clause from Technical Specification 4.0.5.a. Specifically, this change 
    would delete the clause ``(g), except where specific written relief has 
    been granted by the Commission pursuant to 10 CFR Part 50, Section 
    50.55a(g)(6)(i).'' The amendment would also make the appropriate 
    changes to the Bases section. In addition, NNECO made changes to Bases 
    Section 3/4.7.7 and 3/4.7.8 to add design basis information and provide 
    clarification of system design and operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards
    
    [[Page 8801]]
    
    consideration, which is presented below:
    
        Pursuant to 10 CFR 50.92, NNECO has reviewed the proposed 
    changes to Technical Specification 4.0.5a and Bases Section 3/4.4.10 
    and has concluded that the changes do not involve a significant 
    hazards consideration (SHC). The basis for this conclusion is that 
    the three criteria of 10 CFR 50.92(c) are not compromised. The 
    proposed changes do not involve an SHC because the changes would 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes would remove the wording ``* * * (g), 
    except where specific written relief has been granted by the 
    Commission pursuant to 10 CFR Part 50, Section 50.55a(g)(6)(i).'' 
    The Inservice Inspection and Testing Programs are described in the 
    technical specifications pursuant to 10 CFR 50.55a. In addition, the 
    proposed changes, in accordance with NUREG-1431 and NUREG-1482, 
    would provide relief to the ASME Code requirement in the interim 
    between the time of submittal of a relief request until the NRC has 
    issued a safety evaluation and granted the relief. The changes being 
    proposed are administrative in nature and do not affect assumptions 
    contained in plant safety analyses, the physical design and/or 
    operation of the plant, nor do they affect any technical 
    specification that preserves safety analysis assumptions. Any relief 
    from the approved ASME Section XI Code requirements will require a 
    10 CFR 50.59 evaluation to ensure no technical specification changes 
    or unreviewed safety questions exist. Therefore, operation of the 
    facility in accordance with the proposed changes would not affect 
    the probability or consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed changes would remove the wording ``* * * (g), 
    except where specific written relief has been granted by the 
    Commission pursuant to 10 CFR Part 50, Section 50.55a(g)(6)(i).'' 
    The Inservice Inspection and Testing Programs are described in the 
    technical specifications pursuant to 10 CFR 50.55a. In addition, the 
    proposed changes, in accordance with NUREG-1431 and NUREG-1482, 
    would provide relief to the ASME Code requirement in the interim 
    between the time of submittal of a relief request until the NRC has 
    issued a safety evaluation and granted relief. The changes being 
    proposed are administrative in nature and will not change the 
    physical plant or the modes of operation defined in the facility 
    license. The changes do not involve the addition or modification of 
    equipment nor do they alter the design or operation of plant 
    systems. Any relief from the approved ASME Section XI Code 
    requirements will require a 10 CFR 50.59 evaluation to ensure no 
    technical specification changes or unreviewed safety questions 
    exist. Therefore, operation of the facility in accordance with the 
    proposed changes would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The proposed changes would remove the wording ``* * * (g), 
    except where specific written relief has been granted by the 
    Commission pursuant to 10 CFR Part 50, Section 50.55a(g)(6)(i).'' 
    The Inservice Inspection and Testing Programs are described in the 
    technical specifications pursuant to 10 CFR 50.55a. In addition, the 
    proposed changes, in accordance with NUREG-1431 and NUREG-1482, 
    would provide relief to the ASME Code requirement in the interim 
    between the time of submittal of a relief request until the NRC has 
    issued a safety evaluation and granted relief. The changes being 
    proposed are administrative in nature and will not alter the bases 
    for assurance that safety-related activities are performed correctly 
    or the basis for any technical specification that is related to the 
    establishment or maintenance of a safety margin. Any relief from the 
    approved ASME Section XI Code requirements will require a 10 CFR 
    50.59 evaluation to ensure no technical specification changes or 
    unreviewed safety questions exist. Therefore, operation of the 
    facility in accordance with the proposed changes would not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
        United States Department of Commerce, National Institute of 
    Standards and Technology, Docket No. 50-184, NIST (formerly known as 
    National Bureau of Standards) Test Reactor or NBSR.
        Date of amendment request: January 17, 1997.
        Description of amendment request: The National Institute of 
    Standards and Technology (NIST) is planning to change the name of the 
    Reactor Radiation Division to the NIST Center for Neutron Research to 
    be headed by a Director. The requested amendment involves a name change 
    only. All functions, responsibilities, and personnel remain the same. 
    The Technical Specification references to the ``Chief, Reactor 
    Radiation Division'' will be changed to Director, NIST Center for 
    Neutron Research in Sections 7.1, 7.2, and 7.3. The Organization Chart 
    in Figure 7.1 will also reflect this change. The Technical 
    Specification references to the ``Reactor Radiation Division'' will be 
    changed to ``NIST Center for Neutron Research'' in Section 7.2.
        Basis for proposed no significant hazards consideration 
    determination: The Commission has provided standards for determining 
    whether a significant hazards consideration exists (10 CFR 50.92(c)). A 
    proposed amendment would not: (1) Involve a significant increase in the 
    probability or consequences of an accident previously evaluated; or (2) 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated; or (3) involve a significant reduction 
    in a margin of safety.
        The change being proposed is a change in the title of the 
    organization and the title of the head of the organization that directs 
    the operation of the reactor. As noted previously, all functions, 
    responsibilities and personnel remain the same. The staff agrees with 
    the licensee's no significant hazards consideration and finds that the 
    mere title changes render a negative response to the three criteria 
    outlined in 10 CFR 50.92(c).
        Local Public Document Room location: N/A.
        Attorney for licensee: N/A
        NRC Project Director: Seymour H. Weiss.
        Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont.
        Date of amendment request: December 10, 1996.
        Description of amendment request: The proposed amendment would move 
    fire protection requirements from the Vermont Yankee Technical 
    Specifications to the Fire Protection Plan and the final safety 
    analysis report (FSAR), in accordance with the guidance in NRC Generic 
    Letters 86-10 and 88-12.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated:
    
    [[Page 8802]]
    
        The proposed changes are administrative in nature and are 
    consistent with the guidance provided in NRC Generic Letters 86-10 
    and 88-12. These changes do not affect the initial conditions or 
    precursors assumed in the FSAR safety analyses. These proposed 
    changes also do not decrease the effectiveness of equipment relied 
    upon to mitigate the previously evaluated accidents. Programmatic 
    controls will continue to assure that fire protection program 
    changes do not reduce the effectiveness of the program to achieve 
    and maintain safe shutdown in the event of a fire.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from an accident previously 
    evaluated:
        The proposed changes do not modify any plant equipment, there is 
    no reduction in fire protection requirements, there is no change in 
    operating procedure and surveillance requirements and no reduction 
    in administrative control or equipment reliability. Therefore, 
    implementation of the proposed change will not affect the design 
    function or configuration of any component, introduce any new 
    operating scenarios, failure modes or accident initiators.
        3. The proposed amendment will not involve a significant 
    reduction in a margin of safety:
        The proposed amendment does not involve a reduction to the Fire 
    Protection Program. The fire protection requirements are simply 
    being relocated to other controlled documents. There are no 
    equipment modifications being proposed, only the location of fire 
    protection requirements, which is administrative in nature.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: R. K. Gad, III, Ropes and Gray, One 
    International Place, Boston, MA 02110-2624.
        NRC Project Director: Patrick D. Milano, Acting Director.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
        Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina.
        Date of amendment request: January 10, 1997.
        Brief description of amendment: The proposed change would revise 
    Technical Specification 4.8.1.1.2 to clarify pressure testing 
    requirements for the isolable and non-isolable portions of the diesel 
    fuel oil piping.
        Date of publication of individual notice in Federal Register: 
    February 5, 1997 (62 FR 5490).
        Expiration date of individual notice: March 6, 1997.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota.
        Date of amendment request: November 6, 1996.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications governing the cooling water system. 
    The changes are proposed to improve plant operation based on 
    operational experience with the vertical motor-driven cooling water 
    pump. The changes are also proposed to incorporate information gathered 
    by the licensee during its self-assessment Service Water System 
    Operational Performance Inspection (SWSOPI) completed in late 1995.
        Date of individual notice in the Federal Register: January 29, 1997 
    (62 FR 4338).
        Expiration date of individual notice: February 28, 1997.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota.
        Date of amendment requests: January 29, 1997.
        Description of amendment requests: The proposed amendments would 
    change the Bases for Technical Specifications and the licensing basis 
    for the Operating Licenses relating to the cooling water system 
    emergency intake line flow capacity. The licensee determined through 
    testing that the emergency intake line flow capacity was less than the 
    design value stated in the Updated Final Safety Analysis Report. The 
    proposed changes reflect the use of operator actions to control cooling 
    water system flow following a seismic event. The proposed changes also 
    reclassify the intake canal for use during a seismic event, which would 
    be an additional source of cooling water during a seismic event.
        Date of individual notice in the Federal Register: February 7, 1997 
    (62 FR 5857).
        Expiration date of individual notice: March 10, 1997. NSHC 
    comments: February 24, 1997.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey Date of amendment request: January 31, 1997.
        Brief description of amendment request: The amendment would make 
    changes to Technical Specification (TS) 3.4.3, ``Relief Valves,'' for 
    Salem Unit 1, and TS 3.4.5, ``Relief Valves,'' for Salem Unit 2, to 
    ensure that the automatic capability of the power operated relief 
    valves to relieve pressure is maintained when these valves are isolated 
    by closure of the block valves.
        Date of publication of individual notice in Federal Register: 
    February 7, 1997 (62 FR 5861).
        Expiration date of individual notice: March 10, 1997.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
        Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2: Hamilton County, Tennessee.
        Date of application for amendments: October 18, 1996.
        Description of amendments request: Amend Technical Specifications 
    to permanently incorporate new requirements associated with steam 
    generator tube inspections and repair. The requirements provide 
    alternate
    
    [[Page 8803]]
    
    steam generator tube plugging criteria at the tube support plate 
    intersections.
        Date of publication of individual notice in the Federal Register: 
    February 11, 1997 (62 FR 6276).
        Expiration date of individual notice: March 13, 1997.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two Creeks: 
    Manitowoc County, Wisconsin.
        Date of amendment requests: September 19, 1996, as supplemented 
    November 18, 1996, and revised January 13 and January 27, 1997.
        Description of amendment requests: The proposed amendments would 
    change Technical Specification requirements related to the low 
    temperature overpressure protection (LTOP) system. Specifically, the 
    reactor coolant system (RCS) temperature below which LTOP is required 
    to be enabled and the temperature below which one high pressure safety 
    injection pump is required to be rendered inoperable would be changed 
    from less than 275 degrees Fahrenheit to less than 355 degrees 
    Fahrenheit. Additionally, the restriction of ``less than the minimum 
    pressurization temperature for the inservice pressure test as defined 
    in Figure 15.3.1-1'' would be deleted and the specific temperature 
    limit of less than 355 degrees Fahrenheit would be specified. The 
    setpoint for the pressurizer power-operated relief valves (PORVs) would 
    be changed from less than or equal to 425 pounds per square inch gage 
    (psig) to less than or equal to 440 psig to allow for instrument 
    inaccuracies and increased margin allowed by the use of American 
    Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code 
    Case N-514. These modified requirements for LTOP ensure that RCS 
    materials meet the requirements of Title 10 of the Code of Federal 
    Regulations, Sec. 50.60, ``Acceptance Criteria for Fracture Prevention 
    Measures for Lightwater Nuclear Power Reactors for Normal Operation,'' 
    (10 CFR 50.60) in accordance with 10 CFR Part 50, Appendices G and H, 
    and in accordance with the exemption granted on January 27, 1997, which 
    allows the use of ASME Code Case N-514 as an acceptable alternative. 
    Finally, editorial changes would be made to rename the ``Overpressure 
    Mitigating System'' to the ``Low Temperature Overpressure Protection 
    System.'' The September 19, 1996, application was previously noticed in 
    the Federal Register on October 1, 1996 (61 FR 51308).
        Date of individual notice in the Federal Register: February 4, 1997 
    (62 FR 5256).
        Expiration date of individual notice: March 6, 1997. NSHC comments 
    February 19, 1997.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
        Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland.
        Date of application for amendments: November 26, 1996.
        Brief description of amendments: The amendments adopt Option B of 
    10 CFR Part 50, Appendix J to require Type B and Type C containment 
    leakage testing to be performed on a performance-based testing 
    schedule.
        Date of issuance: February 11, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 219 and 196.
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 2, 1997 (62 FR 
    123).
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated February 11, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
        Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts.
        Date of application for amendment: April 25, 1996, as supplemented 
    December 23, 1996.
        Brief description of amendment: The amendment will revise the 
    definition of Operable-Operability, revise Technical Specifications 
    (TSs) and associated Bases Section for TS 3.9.B.2 and 3.9.B.3, 
    ``Auxiliary Electrical System,'' TS 3.4.B.1, ``Standby Liquid Control 
    System,'' TSs 3.7.b.1.a, c, and e, and 3.7.b.2.a, c, and e, ``Standby 
    Gas Treatment System and Control Room High Efficiency Air Filtration 
    System,'' and TSs. 4.5.F.1, ``Core and Containment Cooling Systems,'' 
    and delete TS 3.7.b.1.f, ``Standby Gas Treatment System and Control 
    Room High Efficiency Air Filtration System.''
        Date of issuance: February 10, 1997.
        Effective date: February 10, 1997.
        Amendment No.: 170.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31172).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
        Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-
    
    [[Page 8804]]
    
    455, Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois.
        Docket Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 
    1 and 2, Will County, Illinois.
        Date of application for amendments: August 2, 1996.
        Brief description of amendments: The amendments eliminate License 
    Condition 2.C.(16) from Facility Operating License NPF-37; License 
    Condition 2.C.(5) from Facility Operating License NPF-66; License 
    Condition 2.C.(6) from Facility Operating License NPF-72 and License 
    Condition 2.C.(5) from Facility Operating License NPF-77 that require 
    the licensee to conduct additional corrosion testing of sleeved steam 
    generator tubes.
        Date of issuance: February 12, 1997.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 85 to NPF-37, 85 to NPF-66, 77 to NPF-72, and 77 to 
    NPF-77.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revise the licenses.
        Date of initial notice in Federal Register: September 25, 1996 (61 
    FR 50340).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 12, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina.
        Date of application for amendments: November 26, 1996, as 
    supplemented December 17, 1996
        Brief description of amendments: The amendments revise Technical 
    Specification 3.8.2.1 to allow a one-time change to replace the 
    existing 125-volt AT&T high specific gravity round cell battery banks 
    with the conventional low specific gravity cell battery banks.
        Date of issuance: February 7, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 172 and 154.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 13, 1996 (61 
    FR 65605).
        The December 17, 1996, letter did not change the scope of the 
    November 26, 1996, application and the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 7, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina 28223-0001.
    
        Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana.
        Date of amendment request: August 29, 1996.
        Brief description of amendment: The amendment revises the Technical 
    Requirements Manual (TRM) to change the reactor pressure vessel 
    surveillance capsule withdrawal schedule for the River Bend Station. 
    The first capsule will be withdrawn at 10.4 effective full power years 
    (EFPY) rather than at 6 EFPY.
        Date of issuance: February 13, 1997.
        Effective date: February 13, 1997.
        Amendment No.: 92.
        Facility Operating License No. NPF-47. The amendment revised the 
    Technical Requirements Manual.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55034) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 13, 1997.
        No significant hazards consideration comments received. No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803.
    
        Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana.
        Date of amendment request: June 27, 1996.
        Brief description of amendment: The amendment modifies TS 3/
    4.3.3.6, ``Accident Monitoring Instrumentation,'' to reflect the 
    Combution Engineering improved Standard Technical Specification (STS) 
    approved and issued as NUREG-1432. This amendment revises the TS to 
    include Accident Monitoring Instrumentation recommended in Regulatory 
    Guide (RG) 1.97, ``Instrumentation for Light-Water-
    Cooled Nuclear Plants to Assess Plant Conditions During and Following 
    an Accident,'' Revision 3.
        Date of issuance: February 12, 1997.
        Effective date: February 12, 1997, to be implemented within 90 
    days.
        Amendment No.: 122.
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    40017).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 12, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana.
        Date of amendment request: July 25, 1996, as supplemented by letter 
    dated January 27, 1997.
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications by modifying TS 3/4.7.4, ``Ultimate Heat 
    Sink,'' to incorporate more restrictive fan operability requirements 
    and lower the maximum allowed basin temperature.
        Date of issuance: February 13, 1997.
        Effective date: February 13, 1997.
        Amendment No.: 123.
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 19, 1996 (61 
    FR 58903).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 13, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida.
        Date of application for amendments: October 30, 1996.
        Brief description of amendments: These amendments revise the St. 
    Lucie Technical Specifications to remove inconsistencies between the 
    definition of Core Alterations and the Applicability, Action and 
    Surveillance requirements of two specifications relating to water level 
    and containment
    
    [[Page 8805]]
    
    isolation systems during refueling operations.
        Date of Issuance: February 10, 1997.
        Effective Date: February 10, 1997.
        Amendment Nos.: 148 and 87.
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64386).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
        Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida.
        Date of application for amendment: October 28, 1996.
        Brief description of amendment: The amendments consist of changes 
    to the Technical Specifications (TS) in response to your applications, 
    both dated October 28, 1996, regarding containment leakage tests and 
    removal of certain component lists from the TS.
        Date of Issuance: February 10, 1997.
        Effective Date: February 10, 1997.
        Amendment Nos.: 149 and 88.
        Facility Operating License No. NPF-16: Amendments revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: (61 FR 64386) December 
    4, 1996. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
        Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida.
        Date of application for amendments: December 17, 1996.
        Brief description of amendments: Revision to Technical 
    Specification (TS) 4.4.10 regarding reactor coolant pump flywheel 
    inspection intervals.
        Date of issuance: February 11, 1997.
        Effective date: February 11, 1997.
        Amendment Nos.: 193 and 187.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: January 10, 1997 (62 FR 
    1476). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 11, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
        Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York.
        Date of application for amendment: July 16, 1996.
        Brief description of amendment: The amendment changes the Technical 
    Specifications to permit the use of 10 CFR Part 50, Appendix J, Option 
    B, Performance-Based Containment Leakage Rate Testing in accordance 
    with the implementation guidance in NRC's Regulatory Guide 1.163 dated 
    September 1995.
        Date of issuance: February 10, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 159.
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52965). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota.
        Date of application for amendments: August 15, 1996.
        Brief description of amendments: The amendments revise the 
    containment cooling systems limiting conditions for operation technical 
    specifications to bring them into conformance with recently completed 
    system analyses by no longer permitting both containment spray pumps to 
    be inoperable at the same time.
        Date of issuance: February 10, 1997.
        Effective date: February 10, 1997, with full implementation within 
    30 days.
        Amendment Nos.: 125 and 117.
        Facility Operating License Nos. DPR-42 and DPR-60: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64388).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania.
        Date of application for amendments: November 25, 1996.
        Brief description of amendments: These amendments revise the 
    wording in TS Section 4.8.1.1.2.e.2 and the associated TS Bases Section 
    3/4.8, to remove the specific reference to the Residual Heat Removal 
    (RHR) pump motor and its corresponding kW rating value, and replace it 
    with wording consistent with that specified in the Improved TS (i.e., 
    NUREG-1433, Revision 1, ``Standard Technical Specifications General 
    Electric Plants,'' dated April 1995).
        Date of issuance: February 4, 1997.
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 121 and 85.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 18, 1996 (61 
    FR 66716).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 4, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania.
        Date of application for amendments: September 27, 1996.
        Brief description of amendments: These amendments increase the 
    reactor enclosure secondary containment maximum inleakage rate, and 
    also impact secondary containment drawdown time and system flow rate 
    assumptions, thereby, affecting charcoal filter bed efficiency and post 
    accident dose analysis.
    
    [[Page 8806]]
    
        Date of issuance: February 11, 1997.
        Effective date: Both units, as of the date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 122 and 86.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64392).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 11, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Philadelphia Electric Company, Docket No. 50-353, Limerick 
    GeneratingStation, Unit 2, Montgomery County, Pennsylvania.
        Date of application for amendment: December 6, 1996, as 
    supplemented by letters dated January 15, and 28, 1997.
        Brief description of amendment: This amendment modifies Technical 
    Specification (TS) Section 2.1 and its associated TS Bases to reflect 
    the change in the Minimum Critical Power Ratio safety limit due to the 
    use of GE13 fuel product line and the cycle-specific analysis performed 
    by General Electric Company (GE), for LGS, Unit 2, Cycle 5.
        Date of issuance: February 12, 1997.
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment No.: 87.
        Facility Operating License No. NPF-85. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 23, 1996 (61 
    FR 67582).
        The January 15, and 28, 1997, letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 12, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey.
        Date of application for amendments: June 10, 1996, as supplemented 
    June 24, July 1, August 13, September 20, and October 17, 1996.
        Brief description of amendments: The amendments change Technical 
    Specifications 3/4.3.3.1, ``Radiation Monitoring Instrumentation,'' and 
    3/4.7.6, ``Control Room Emergency Air Conditioning System,'' to reflect 
    a control room design in which the common Unit 1 and Unit 2 control 
    room envelope is supplied by 2 one hundred percent capable Control Room 
    Emergency Air Conditioning System trains.
        Date of issuance: February 6, 1997.
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 190 and 173.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 24, 1996 (61 FR 
    32468) The June 24, July 1, August 13, September 20, and October 17, 
    1996, letters provided clarifying information that did not change the 
    initial proposed no significant hazards consideration determination nor 
    expand the scope of the initial submittal as described in the initial 
    notice.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 6, 1997.
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
        Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, 
    New Jersey.
        Date of application for amendments: May 31, 1996, as supplemented 
    December 23, 1996.
        Brief description of amendments: The amendments change the 
    Technical Specification to (1) Revise the reactor vessel level 
    indication system action statements, (2) revise the channel calibration 
    definition, and (3) delete a requirement to install la jumper in the 
    auxiliary feedwater actuation logic.
        Date of issuance: February 6, 1997.
        Effective date: Both units, as of its date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 191 and 174.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 17, 1996 (61 FR 
    30641).
        The December 23, 1996, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 6, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
        Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, 
    Alabama.
        Date of amendments request: November 15, 1996.
        Brief Description of amendments: The amendments replace Containment 
    Systems TS 3.6.2.2 for the Spray Additive System, with a new Emergency 
    Core Cooling Systems (ECCS) TS 3.5.6 for the ECCS Recirculation Fluid 
    pH Control System.
        Date of issuance: February 3, 1997.
        Effective date: As of the date of issuance to be implemented prior 
    to Mode 4 for Unit 1 following the spring 1997 refueling outage; for 
    Unit 2 following the spring 1998 refueling outage.
        Amendment Nos.: 123 and 118.
        Facility Operating License Nos. NPF-2 and NPF-8: Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: December 18, 1996 (61 
    FR 66718).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 3, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
        Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio.
        Date of application for amendment: August 7, 1996.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 1.0, ``Definitions,'' by defining a refueling 
    interval to be [less than or equal to] 730 days; and revises TS 3/4.0, 
    ``Applicability,'' TS 3/4.6.2.1, ``Containment Systems--
    Depressurization and Cooling Systems--Containment Spray System,'' and 
    TS 3/4.6.3.1, ``Containment Systems--
    
    [[Page 8807]]
    
     Containment Isolation Valves,'' to reflect performing surveillance 
    tests during a refueling interval rather than every 18 months.
        Date of issuance: February 10, 1997.
        Effective date: February 10, 1997, to be implemented not later than 
    120 days after issuance.
        Amendment No.: 213.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52970).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 10, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606.
        Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio.
        Date of application for amendment: September 12, 1996.
        Brief description of amendment: The amendment revised Technical 
    Specifications (TS) 3/4.1.3.4, ``Reactivity Control Systems--Rod Drop 
    Time,'' and TS 3/4.5.2, ``Emergency Core Cooling Systems--Tavg [greater 
    than or equal to] 280 deg.F,'' to change the surveillance test interval 
    from every 18 months to each refueling interval ([less than or equal 
    to] 730 days, nominally 24 months). Additionally, the amendment removed 
    a footnote for TS 4.5.2.b that is no longer applicable.
        Date of issuance: February 11, 1997.
        Effective date: February 11, 1997, to be implemented not later than 
    120 days over issuance.
        Amendment No.: 214.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 11, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606.
    
        Dated at Rockville, Maryland, this 19th day of February 1997.
    
        For the Nuclear Regulatory Commission.
    Jack W. Roe,
    Director, Division of Reactor Projects--III/IV, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 97-4573 Filed 2-25-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
02/26/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-4573
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
8790-8807 (18 pages)
PDF File:
97-4573.pdf