97-4701. Baltimore Gas and Electric Company; Notice of Consideration of Issuance of Amendment to Facility Operating License, Proposed No Significant Hazards Consideration Determination, and Opportunity for a Hearing  

  • [Federal Register Volume 62, Number 38 (Wednesday, February 26, 1997)]
    [Notices]
    [Pages 8780-8783]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-4701]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-317 and 50-318]
    
    
    Baltimore Gas and Electric Company; Notice of Consideration of 
    Issuance of Amendment to Facility Operating License, Proposed No 
    Significant Hazards Consideration Determination, and Opportunity for a 
    Hearing
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of an amendment to Facility Operating License Nos. 
    DPR-53 and DPR-69 issued to Baltimore Gas and Electric Company, for 
    operation of the Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, 
    located in Calvert County, Maryland.
        The proposed amendment revises the Technical Specifications (TSs) 
    to reduce the minimum Reactor Coolant System (RCS) total flow rate from 
    370,000 gpm to 340,000 gpm; reduce the Reactor Protective 
    Instrumentation trip setpoint for Reactor Coolant Flow--Low from 
    greater than or equal to 95% to greater than or equal to 92% of design 
    reactor coolant flow; adjust the reactor core thermal margin safety 
    limit lines to reflect the reduced RCS flow rate; and reduce the lift 
    setting range for the eight Main Steam Safety Valves (MSSVs) with the 
    highest allowable lift setting from the current range of 935 to 1065 
    psig to a more restrictive range of 935 to 1050 psig. In addition to 
    the changes to the TSs necessary to support an increased number of 
    plugged SG tubes, reanalysis of the accident analyses affected by this 
    change identified an Unreviewed Safety Question (USQ) associated with 
    these changes. The USQ results from the determination that the Main 
    Steam Line Break (MSLB) and Seized Rotor Event analyses involve an 
    increased percentage of failed fuel cladding. Finally, three reanalyzed 
    events (MSLB, Loss of Coolant Flow, and Boron Dilution) will require 
    Nuclear Regulatory Commission (NRC) approval due to changes to the 
    methodology or assumptions used to analyze these events.
        Before issuance of the proposed license amendment, the Commission 
    will have made findings required by the Atomic Energy Act of 1954, as 
    amended (the Act) and the Commission's regulations.
        The Commission has made a proposed determination that the amendment 
    request involves no significant hazards consideration. Under the 
    Commission's regulations in 10 CFR 50.92, this means that operation of 
    the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. As 
    required by 10 CFR 50.91(a), the licensee has provided its analysis of 
    the issue of no significant hazards consideration, which is presented 
    below:
    
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed amendment defines changes to the operating licenses 
    for Calvert Cliffs Nuclear Power Plant, Units 1 and 2, necessary to 
    support increased steam generator tube plugging. The effects of 
    increased steam generator tube plugging include reduced steam 
    generator pressure and RCS flow rate, and increased core outlet (hot 
    leg) temperature. The Technical Specification changes necessary to 
    account for these effects are reducing the minimum RCS total flow 
    rate from 370,000 gpm to 340,000 gpm; reducing the Limiting Safety 
    System Setting for reactor coolant flow trip function from greater 
    than or equal to 95% to greater than or equal to 92% of design 
    reactor coolant flow; revising the Reactor Core Thermal Safety Limit 
    lines to indicate operation at the lower reactor coolant flow rate; 
    and decreasing the maximum allowable lift settings for the eight 
    highest set Main
    
    [[Page 8781]]
    
    Steam Safety Valves from 1065 psig to 1050 psig. The Design Basis 
    Events (DBEs) affected by these changes were reanalyzed to determine 
    if the effects of increased steam generator tube plugging, and the 
    associated changes to the Technical Specifications, could result in 
    exceeding the acceptance criteria applicable to each of these 
    events. Although it was determined that the DBE acceptance criteria 
    would not be exceeded as a result of increased steam generator tube 
    plugging, the analyses for the Main Steam Line Break and Seized 
    Rotor Events indicated an increased percentage of fuel cladding 
    failure as a result of the lower RCS total flow rate; therefore, it 
    was determined that this activity involves a USQ.
        Technical Specification 2.1.1 will be changed to establish more 
    restrictive limits on core thermal power and reflect a lower minimum 
    RCS flow of 340,000 gpm. Making the core thermal power limits more 
    restrictive does not initiate a change to plant conditions that 
    would affect other plant components. Therefore, the probability of a 
    previously evaluated accident is not significantly increased. 
    Additionally, the Limiting Conditions for Operation and Limiting 
    Safety System Settings based on these limits remain adequately 
    conservative or will be changed in the Core Operating Limits Report, 
    as appropriate. Therefore, the consequences of a previously 
    evaluated accident are not significantly increased.
        Technical Specification 2.2 will be changed to reduce the 
    Reactor Coolant Flow--Low reactor trip setpoint from [greater than 
    or equal to] 95% to [greater than or equal to] 92%, thereby 
    providing additional operating margin to this trip setpoint and the 
    associated pre-trip alarm. Reducing this setpoint does not initiate 
    a change to plant conditions that would affect other plant 
    components. Therefore, the probability of a previously evaluated 
    accident is not significantly increased.
        As demonstrated by the revised Loss of Coolant Flow analysis, 
    the proposed Reactor Coolant Flow--Low reactor trip setpoint will 
    continue to provide adequate core protection. A trip setpoint of 
    [greater than or equal to] 92% ensures fuel is not damaged, and the 
    site boundary dose remains a small fraction of the 10 CFR Part 100 
    guidelines. Therefore, the consequences of a previously evaluated 
    accident are not significantly increased.
        Technical Specification 3.2.5.c will be changed to reduce the 
    minimum RCS total flow rate from 370,000 gpm to 340,000 gpm. This 
    change reduces the core heat removal rate and slightly increases the 
    core outlet and average coolant temperatures. This change involves a 
    USQ, as the Main Steam Line Break and Seized Rotor Event analyses 
    have indicated an increase in the number of failed fuel pins during 
    these events as a result of reducing the initial RCS flow rate. The 
    probability of malfunction of equipment important to safety (i.e., 
    fuel pin cladding) during these accidents increases. However, this 
    malfunction is not an accident initiator. Rather, it is a 
    consequence of an accident. Therefore, the probability of a 
    previously evaluated accident is not significantly increased. The 
    consequences of the Main Steam Line Break and Seized Rotor Events 
    are not significantly increased, as the results of the analyses of 
    these events are within the current acceptance criteria established 
    by the NRC.
    
        Analyses and evaluations have been performed to demonstrate that 
    the new flow and temperature conditions are acceptable:
    
        Fuel and core performance remain within acceptable limits. 
    Analysis and evaluation of fuel mechanical design, core physics, 
    parameters, fuel pin performance, fuel assembly thermal/hydraulic 
    performance, and fuel pin corrosion all demonstrate acceptable 
    results.
        The effect of the slightly elevated core outlet and average 
    coolant temperature on the structural integrity of the RCS is 
    acceptable. The RCS penetration inspection program and the steam 
    generator tube inspection program will continue to identify and 
    repair or isolate Alloy 600 cracks prior to inservice failure of 
    these components. The stress analysis for the reactor vessel and 
    piping remain bounding.
        The performance of control systems (i.e., feedwater, pressurizer 
    level, and pressurizer pressure) will maintain RCS and steam 
    generator parameters within appropriate limits by periodic 
    adjustment, as necessary. Reactor coolant pump operation will be 
    maintained within acceptable limits by periodic adjustment of the 
    operating curves.
    
        Therefore, the probability of a previously evaluated accident is 
    not significantly increased.
        Analyses and evaluations of the DBEs have been performed 
    demonstrating that the NRC acceptance criteria for these events are 
    met. The revised analyses and evaluations consider reduced RCS flow, 
    increased reactor coolant temperature, and increased steam generator 
    tube plugging conditions.
    
        The results of analyses and evaluations of the Postulated 
    Accidents demonstrate that the site boundary dose is within 10 CFR 
    Part 100 guidelines and the core geometry remains coolable. Loss-of-
    Coolant Accident analysis results meet the acceptance criteria 
    stipulated in 10 CFR 50.46(b).
        The results of analyses and evaluations of Anticipated 
    Operational Occurrences demonstrate that fuel parameters do not 
    exceed the specified acceptable fuel design limits and site boundary 
    dose is a small fraction of 10 CFR Part 100 guidelines. Primary and 
    secondary system pressure remain below the pressure upset limits for 
    the RCS and steam generators, respectively.
    
        Therefore, the consequences of a previously evaluated accident are 
    not significantly increased.
    
        Technical Specification 4.7.1.1. will be changed to reduce the 
    maximum allowable lift setting for the eight Main Steam Safety 
    Valves with the highest lift setpoint. This change will place more 
    restrictive limits on the allowable range of lift settings for these 
    eight valves. The allowable range of lift settings for the proposed 
    change is also allowed by current Technical Specification. 
    Therefore, the probability of a previously evaluated accident 
    occurring is not significantly increased.
        The revised safety analyses will credit the highest lift setting 
    for these eight valves as being 1050 psig. The more restrictive 
    limit on the maximum lift setting is required in order to make this 
    Technical Specification consistent with the revised safety analyses. 
    Analyses performed assuming the proposed maximum lift setting for 
    these valves demonstrates that secondary system pressure does not 
    exceed 110% of the system design pressure. Therefore, the 
    consequences of a previously evaluated accident are not 
    significantly increased.
        Therefore, operation of the facility in accordance with this 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed amendment revises limiting parameters to assure 
    safe operation commensurate with the effects of steam generator tube 
    plugging, and will not change the modes of operation defined in the 
    facility license. The analysis of transients associated with steam 
    generator malfunctions are part of the design and licensing bases. 
    This change does not add any new equipment, modify any interfaces 
    with any existing equipment, or change the equipments's function, or 
    the method of operating the equipment. The proposed change does not 
    change plant conditions in a manner which could affect other plant 
    components. Reactor core, RCS, and steam generator parameters remain 
    within appropriate design limits during normal operation.
        Therefore, the proposed change could not cause any existing 
    equipment to become an accident initiator.
        Therefore, the proposed change does not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The margins of safety associated with this change are defined in 
    the fuel and core-related analyses, the Alloy 600 stress corrosion 
    cracking evaluation, the RCS structural evaluation, the operational 
    evaluation, and in each of the transient and accident analyses 
    affected by the increased steam generator tube plugging.
        Reanalysis of the fuel and core-related analyses for fuel 
    mechanical design, core physics, fuel performance, thermal 
    hydraulics, and fuel rod corrosion verified that the fuel and core 
    performance will remain within acceptable limits and will be bounded 
    by the current assumptions for fuel performance in the transient and 
    accident analyses. The Alloy 600 RCS penetration inspection program 
    and the steam generator tube inspection program will continue to 
    find and repair Alloy 600 cracks at the slightly elevated core exit 
    temperature prior to any postulated inservice failure of these 
    components. The stress analyses performed for the reactor vessel and 
    piping remain bounding for the slightly elevated core exit
    
    [[Page 8782]]
    
    temperature. Additionally, the performance of non-safety-related 
    control systems remains adequate to maintain RCS and steam generator 
    parameters within appropriate operating limits. Therefore, the 
    margins of safety associated with the physical and operational 
    effects of this change will not be significantly reduced.
        An evaluation of the affected DBEs confirmed that the 
    established acceptance criteria for specified acceptable fuel design 
    limits, primary and secondary system over-pressurization, 10 CFR 
    50.46(b), Acceptance Criteria for Emergency Core Cooling Systems for 
    Light-Water Nuclear Power Reactors, and potential radiation dose 
    during accidents have been completed in support of this license 
    amendment request. The evaluation concludes that, when considering 
    the proposed Limiting Safety System Setting for the Reactor Coolant 
    Flow--Low trip, Limiting Conditions for Operation for RCS total flow 
    rate, and reduced lift settings for eight Main Steam Safety Valves 
    per unit, all applicable acceptance limits are met. Furthermore, the 
    USQ resulting from the reduced RCS total flow rate does not 
    represent a reduction in the margin of safety, as the site boundary 
    dose calculated in the affected DBE analyses is within the current 
    established radiation dose limits and the core geometry remains 
    coolable. Therefore, the margins of safety associated with the 
    transient and accident analyses affected by this change will not be 
    significantly reduced.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received. 
    Should the Commission take this action, it will publish in the Federal 
    Register a notice of issuance and provide for opportunity for a hearing 
    after issuance. The Commission expects that the need to take this 
    action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland, from 7:30 a.m. to 
    4:15 p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC.
        The filing of requests for hearing and petitions for leave to 
    intervene is discussed below.
        By March 28, 1997 the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC, and at the local public 
    document room located at the Calvert County Library, Prince Frederick, 
    Maryland 20678. If a request for a hearing or petition for leave to 
    intervene is filed by the above date, the Commission or an Atomic 
    Safety and Licensing Board, designated by the Commission or by the 
    Chairman of the Atomic Safety and Licensing Board Panel, will rule on 
    the request and/or petition; and the Secretary or the designated Atomic 
    Safety and Licensing Board will issue a notice of hearing or an 
    appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
    
    [[Page 8783]]
    
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to S. Singh Bajwa: petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-0001, and to Jay E. 
    Silbert, Esquire, Shaw, Pittman, Potts and Trowbridge, 2300 N Street, 
    NW., Washington, DC, 20037 attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for hearing will not 
    be entertained absent a determination by the Commission, the presiding 
    officer or the presiding Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment dated January 31, 1997, as supplemented 
    February 13, 1997, which is available for public inspection at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC, and at the local public document room located at 
    the Calvert County Library, Prince Frederick, Maryland 20678.
    
        Dated at Rockville, Maryland, this 20th day of February 1997.
    
        For the Nuclear Regulatory Commission.
    Alexander W. Dromerick,
    Senior Project Manager, Project Directorate I-1, Division of Reactor 
    Projects--I/II, Office of Nuclear Reactor Regulation.
    [FR Doc. 97-4701 Filed 2-25-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
02/26/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-4701
Pages:
8780-8783 (4 pages)
Docket Numbers:
Docket Nos. 50-317 and 50-318
PDF File:
97-4701.pdf