96-4342. Biweekly Notice, Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 40 (Wednesday, February 28, 1996)]
    [Notices]
    [Pages 7542-7568]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-4342]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice, Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from February 5, 1996, through February 15, 1996. 
    The last biweekly notice was published on February 14, 1996 (61 FR 
    5809). 
    
    [[Page 7543]]
    
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By March 29, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public 
    
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    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: December 20, 1995.
        Description of amendments request: The proposed amendment would 
    change the instrumentation setpoint for the reactor trip and main steam 
    isolation signal (MSIS) actuation on low steam generator pressure from 
    greater than or equal to 919 psia with an allowable value of greater 
    than or equal to 911 psia to greater than or equal to 895 psia with an 
    allowable value of greater than or equal to 890 psia.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed amendment does not involve any change to the method 
    of operation of any plant equipment that is used to mitigate the 
    consequences of an accident. The proposed change only affects the 
    instrument setpoint for steam generator low pressure reactor trip 
    and MSIS actuation. The proposed setpoint meets the requirement of 
    ensuring a reactor trip and MSIS actuation prior to steam generator 
    pressure reaching the analytical limits even under worst-case 
    accident conditions. Thus, the proposed change does not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The proposed amendment does not alter any of the assumptions or 
    bounding conditions currently in the UFSAR [updated final safety 
    analysis report] and meets the requirement of ensuring a reactor 
    trip and MSIS actuation prior to steam generator pressure reaching 
    the analytical setpoint under worst-case accident conditions. As a 
    result, the proposed amendment does not involve a significant 
    increase in the consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not involve any change to the method of 
    operation of any plant equipment that is used to mitigate the 
    consequences of an accident. Accordingly, no new failure modes have 
    been defined for any plant system or component important to safety 
    nor has any new limiting failure been identified as a result of the 
    proposed change. The intent of the proposed change is to increase 
    the margin between normal operating parameters and trip setpoints. 
    This minimizes the possibility of unnecessary challenges to safety 
    systems improving the safety of operation. The method of protecting 
    the facility for an excess steam demand event remains unchanged and 
    therefore, the amendment does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change is the implementation of a setpoint value 
    which was derived using methodologies endorsed by Revision 2 of NRC 
    Regulatory Guide 1.105, ``Instrument Setpoints.'' The new setpoint 
    ensures that sufficient margin exists below the full load operating 
    value for steam pressure so as not to interfere with normal plant 
    operation, but still high enough to provide the required protection 
    (reactor trip and main steam line isolation) in the event of an 
    excessive steam demand event. The new setpoint ensures that safety 
    margins are maintained within the results of existing calculations. 
    The margin of safety between the analyzed trip value and the point 
    at which safety analysis results become unacceptable remain 
    unchanged since the analytical setpoints are not affected by the 
    amendment. The new setpoint resulted from the reduced instrument 
    uncertainty and will ensure that the reactor trip and MSIS actuation 
    on low steam generator pressure will occur before the analyzed value 
    and hence, this change does not involve a significant reduction in 
    the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999.
        NRC Project Director: William H. Bateman.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: January 5, 1996.
        Description of amendments request: The proposed amendment would 
    revise paragraph 2.C.(1) of the operating licenses and Section 1.26 of 
    the TS for each of the three PVNGS Units to increase the authorized 100 
    percent reactor core power (rated thermal power) from 3800 megawatts 
    thermal (Mwt) to 3876 Mwt, an increase of 2 percent. The proposed 
    amendment would also revise TS 4.1.1.4, TS 3.1.3.4, and TS 3.2.6 
    (Figure 3.2-1) to lower the allowable reactor coolant system cold leg 
    temperature limits for each of the three PVNGS Units, and revise TS 
    3.4.2.1 and TS 3.4.2.2 to lower the pressurizer safety valve setpoints 
    for Units 1 and 3 to support the increased power operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed amendment does not change the method of operation 
    or modify the plant configuration other than minor changes in 
    equipment setpoints. Thus no increase in the probability of an 
    accident is created by this amendment. System and programmatic 
    reviews have been performed on the nuclear 
    
    [[Page 7545]]
    steam supply system controls, reactor coolant system mechanical, steam 
    generator mechanical, balance of plant systems, and fire protection, 
    equipment qualification, and probabilistic risk assessment programs. 
    The conclusion of these reviews was that operation in accordance 
    with the changes proposed in this amendment was acceptable and posed 
    no significant risk to the health and safety of the public. The 
    analyses supporting this amendment demonstrate that the consequences 
    of events using the changes specified in the amendment are within 
    the criteria which are the current licensing basis for the PVNGS 
    Units. Therefore the amendment, as proposed, does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment does not modify the configuration of the 
    units except for minor equipment setpoints. No equipment changes and 
    no new methods of plant operation are being proposed, therefore, no 
    new failure modes are introduced by the proposed amendment. The 
    setpoint changes proposed have been evaluated and shown to be 
    acceptable in providing their design function. The increased rated 
    thermal power and associated changes have been incorporated into the 
    safety analysis performed in support of this amendment request and 
    the results have been shown to be similar to those previously 
    obtained. No possibility of a new or different kind of accident from 
    any accident previously evaluated will be created as a result of the 
    proposed amendment.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The changes proposed were evaluated in the safety analysis 
    performed to justify the amendment request. Although the 
    consequences of some events increased slightly, the results continue 
    to meet the criteria which form the PVNGS licensing basis. The 
    programmatic and system reviews provide further assurance of the 
    capability of the units to continue to operate safely with the 
    changes proposed in this amendment. Therefore the amendment does not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999.
        NRC Project Director: William H. Bateman.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: January 29, 1996.
        Description of amendment request: The proposed change would revise 
    the technical specifications (TS) table 4.1-3, item 4 to change the 
    frequency of main steam safety valve (MSSV) testing to that specified 
    in NUREG-1431, the improved ``Standard Technical Specifications, 
    Westinghouse Plants'' (one third of the MSSVs each refueling outage). 
    In addition, the licensee proposed adding the MSSV test acceptance 
    requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Neither the valves' nor the system's configuration or functions 
    are being altered. The valves' setpoints and their ``as-left'' 
    range, +/-1%, will not be changed. The changes are to the testing 
    frequency and the ``as found'' tolerance of the MSSV setpoint.
        The proposed changes in testing frequency and the higher 
    tolerance are in the less conservative direction, but are not 
    significant for several reasons. First, the new standards are based 
    on the American Society of Mechanical Engineers (ASME) Boiler and 
    Pressure Vessel Code. The new standards have been accepted by the 
    nuclear industry and the NRC, and are referenced in the improved 
    Standard Technical Specifications. Based on a discussion with the H. 
    B. Robinson Steam Electric Plant (HBRSEP), Unit No. 2 MSSV 
    manufacturer (i.e., Crosby), HBRSEP, Unit No. 2 has not experienced 
    more problems with the Crosby MSSVs than the nuclear industry in 
    general, thus, the new level of safety will be equivalent to that of 
    the nuclear industry. Second, if a MSSV does fail the surveillance 
    test, the proposed TS will require additional MSSVs to be tested. 
    This requirement provides assurance that testing will reveal 
    possible generic problems. The impact of the tolerance on the 
    Chapter 15 accidents was analyzed and found to be within acceptable 
    limits.
        Since no Updated Final Safety Analysis Report (UFSAR) Chapter 15 
    accident analysis is significantly impacted by the proposed changes, 
    there would be no increase in the consequences of an accident 
    previously evaluated. The testing in accordance with the ASME Boiler 
    and Pressure Vessel Code will provide an adequate level of assurance 
    that the MSSVs will be able to perform their intended function; 
    therefore the probability of a previously evaluated accident is not 
    increased.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        No new systems or equipment are involved with the proposed 
    changes; and the plant's configuration and operational procedures 
    are unaffected. Since the proposed changes do not impact the plant's 
    operation, it can not create a new or different kind of accident.
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety.
        The change in testing frequency is in a less conservative 
    direction, but it is based on the ASME Code and the improved 
    Standard Technical Specifications. Since HBRSEP, Unit No. 2 has not 
    experienced a greater number of failures associated with these MSSVs 
    than the nuclear industry in general, the decrease in the MSSV 
    testing frequency will not significantly impact the margin of 
    safety. Also, analyses have been performed that demonstrate that the 
    impact of the setpoint tolerance change on the UFSAR Chapter 15 
    accident analysis results is not significant. Therefore, the 
    proposed changes do not involve a significant reduction in a margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: David B. Matthews.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: January 31, 1996.
        Description of amendment request: The proposed change would revise 
    the Technical Specifications section 4.4 to allow the use of 10 CFR 
    Part 50, Appendix J, Option B, Performance-Based Containment Leakage 
    Rate Testing. A new TS section 6.12 is proposed to describe the 
    containment leakage rate testing program, committing to meet 10 CFR 
    50.54(o) and 10 CFR Part 50, Appendix J, Option B for type A tests; and 
    to meet 10 CFR part 50, Appendix J, Option A, for types B and C tests. 
    The bases would be changed to reflect the proposed changes. 
    
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        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed change does not involve a significant hazards 
    consideration for the following reasons.
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The HBRSEP [H. B. Robinson Steam Electric Plant], Unit No. 2 
    Type A testing history provides substantial justification for the 
    proposed test schedule change to one test in a 10 year period. Three 
    Structural Integrity Tests (SITs) and seven Integrated Leak Rate 
    Tests (ILRTs) have been performed with acceptable results. Previous 
    testing has affirmed the acceptable reliability of the containment 
    structure to minimize leakage as designed, and provides assurance 
    that its performance to continuously function as designed is not 
    challenged due to this test schedule extension to once in 10 years.
        Therefore, this proposed change to the TS that revises the Type 
    A testing frequency does not involve an increase in the probability 
    of an accident previously evaluated.
        This proposed change to revise the test schedule frequency does 
    not impact nor alter the design of any system, structure or 
    component. The limit on allowable leakage is not increased. Type A 
    testing provides periodic verification of the leak tight integrity 
    of the containment and the systems and components that penetrate the 
    containment structure.
        NUREG-1493, ``Performance-Based Containment Leak-Test Program,'' 
    provides the technical basis for the NRC's rulemaking to revise 
    containment leakage testing requirements for nuclear power reactors 
    in 10 CFR 50, Appendix J. Section 10.1.2 of NUREG-1493, ``Summary of 
    Technical Findings, Leakage-Testing Intervals,'' states the 
    following.
        1. Reducing the frequency of Type A tests (ILRTs) from the 
    current three per 10 years to one per 20 years was found to lead to 
    an imperceptible increase in risk. The estimated increase in risk is 
    very small because ILRTs identify only a few potential containment 
    leakage paths that cannot be identified by Type B and C testing, and 
    the leaks found by Type A tests have been only marginally above 
    existing requirements.
        2. Given the insensitivity of risk to containment leakage rate 
    and the small fraction of leakage paths detected solely by Type A 
    testing, increasing the interval between ILRTs is possible with 
    minimal impact on public risk.
        Therefore, based on the previous Type A test results, the 
    proposed change does not involve a significant increase in the 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change only incorporates the performance based 
    testing approach authorized in 10 CFR 50, Appendix J, Option B, and 
    is justified based on previous plant-specific Type A test results. 
    Plant structures, systems, and components will not be operated in a 
    different manner as a result of this proposed change and no physical 
    modifications to equipment are involved. The interval extensions 
    allowed by Option B of 10 CFR 50, Appendix J, do not have the 
    potential for creating the possibility of new or different type of 
    accidents from those previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The proposed change does not change the allowable leak rate from 
    the containment, it only allows an extension of the interval between 
    the performance of Type A leak rate testing. NUREG-1493, which 
    provides the technical basis for the NRC's rulemaking to revise 
    containment leakage testing requirements for nuclear power reactors 
    in 10 CFR 50, Appendix J. Section 10.1.2 of NUREG-1493, ``Summary of 
    Technical Findings, Leakage-Testing Intervals,'' states the 
    following.
        ``1. Reducing the frequency of Type A tests (ILRTs) from the 
    current three per 10 years to one per 20 years was found to lead to 
    an imperceptible increase in risk. The estimated increase in risk is 
    very small because ILRTs identify only a few potential containment 
    leakage paths that cannot be identified by Type B and C testing, and 
    the leaks found by Type A tests have been only marginally above 
    existing requirements.
        2. Given the insensitivity of risk to containment leakage rate 
    and the small fraction of leakage paths detected solely by Type A 
    testing, increasing the interval between ILRTs is possible with 
    minimal impact on public risk.''
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: David B. Matthews.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: January 29, 1996.
        Description of amendment request: The proposed change would revise 
    the technical specifications (TS) to: (1) add TS 4.6.1.5 to provide 
    criteria for 24-hour full-load testing of the emergency diesel 
    generators (EDGs) to be performed during each refueling outage; (2) 
    revise TS 4.6.1.2 to allow testing of the EDG protective bypasses 
    listed in TS 3.7.1.d to be done independent of the safety injection or 
    loss of offsite power testing; and (3) revise TS 4.6.1.3 to include the 
    EDG protective bypass inspection and a requirement to inspect the EDGs 
    at least once every refueling outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed changes do not involve a significant hazards 
    consideration for the following reasons.
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes do not involve a significant increase in 
    the probability of an accident previously evaluated. The proposed 
    changes require additional testing of the EDGs and will change the 
    requirement for when the protective bypasses are tested. The 
    function of the EDGs remains unchanged. Since the additional testing 
    involves the EDGs, which are required to mitigate an accident and 
    are not involved in the initiation of an accident, the proposed 
    changes will not increase the probability of an accident.
        The proposed changes do not involve a significant increase in 
    the consequences of an accident previously evaluated. The proposed 
    changes require additional testing to verify the reliability of the 
    EDGs and to show the EDGs can withstand maximum accident loading 
    conditions. The proposed changes will also require the testing of 
    the EDG protective bypasses to be accomplished during EDG outages 
    and not during the SI/LOOP testing during a refueling outage. The 
    ability of the EDGs to perform their accident mitigation function 
    remains unchanged. Therefore, the proposed changes will not increase 
    the consequences of an accident.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not create the possibility of a new kind 
    of accident from any previously evaluated. The proposed changes are 
    an enhancement to the EDG testing requirements. The most significant 
    change will require additional testing of the EDGs to demonstrate 
    adequate reliability and to determine if the EDGs can withstand 
    maximum accident loading conditions. The remaining changes will 
    augment the TS to allow on-line EDG inspections and testing. Since 
    the function of the EDGs remains unchanged and they are not the 
    initiator of an accident, the proposed changes will not 
    
    [[Page 7547]]
    create the possibility of a new kind of accident from any previously 
    evaluated.
        The proposed changes do not create the possibility of a 
    different kind of accident from any accident previously evaluated. 
    The proposed changes require additional testing of the EDGs (i.e., 
    the 24 hour full-load test) and revise the requirement for testing 
    the EDG protective bypasses during the SI/LOOP testing. The 
    additional testing of the EDGs will demonstrate sufficient 
    reliability and determine if the EDGs can withstand maximum accident 
    loading conditions. The EDG protective bypasses will be statically 
    tested during an EDG outage thus preventing possible damage to 
    equipment from a transient if the protective bypass fails. The 
    function of the EDGs remains unchanged by these proposed changes. 
    Since the EDGs are required to mitigate an accident and are not the 
    initiators of an accident, the proposed changes will not create a 
    different kind of accident from any kind of accident previously 
    evaluated.
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety.
        The proposed changes do not reduce the margin of safety as 
    defined in the TS. The proposed changes are being submitted as an 
    enhancement to the testing requirements outlined in the TS. The 
    changes include additional testing, revising the requirement to test 
    the engine protective bypasses during the SI/LOOP testing and 
    clarification of the periodicity of inspecting the EDGs. The 
    additional testing demonstrates increased reliability and determines 
    that the EDGs can cope with maximum accident loading. The remaining 
    proposed changes provide clarification as to when the EDG 
    inspections and testing are required. The ability of the EDGs to 
    perform their function will not be reduced. Therefore, the margin of 
    safety will not be reduced by the proposed changes.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: David B. Matthews.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois; Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of amendment request: December 6, 1995.
        Description of amendment request: The proposed amendment would 
    change the technical specifications of these plants to incorporate 10 
    CFR Part 50, Appendix J, ``Primary Reactor Containment Leakage Testing 
    for Water-Cooled Power Reactors'', Option B.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        ComEd proposes to revise Byron Nuclear Power Station, Units 1 
    and 2 (Byron), and Braidwood Nuclear Power Station, Units 1 and 2 
    (Braidwood) Technical Specification (TS) Section 3/4.6.1, ``Primary 
    Containment,'' and the associated Bases to reflect recent changes to 
    Appendix J to 10 CFR 50, ``Primary Reactor Containment Leakage 
    Testing for Water-Cooled Power Reactors.'' The proposed revisions 
    include:
        1. Adding TS Definitions 1.15.a for the maximum allowable 
    primary containment leakage rate (La) and 1.20.a for the 
    maximum calculated primary containment pressure (Pa). The 
    redundant definitions throughout TS Section 3/4.6.1 are deleted,
        2. Adding numerous statements throughout TS Section 3/4.6.1 that 
    leak rate testing is performed in accordance with Regulatory Guide 
    (RG) 1.163, Revision 0, ``Performance-Based Containment Leak-Test 
    Program,'' and its referenced documents,
        3. Deleting TS requirements that are taken verbatim from 10 CFR 
    50, Appendix J. The specific requirements will be placed in the 
    containment leakage rate test program in accordance with RG 1.163, 
    and its referenced documents, and
        4. Clarifying Technical Specification Surveillance Requirement 
    (TSSR) 4.6.1.1.a for consistency with NUREG-1431, Revision 1, 
    ``Standard Technical Specifications for Westinghouse Plants.''
        A. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        10 CFR 50, Appendix J, has been amended to include provisions 
    regarding performance-based leakage testing requirements (Option B). 
    Option B allows plants with satisfactory Integrated Leak Rate 
    Testing (ILRT) performance history to reduce the Type A testing 
    frequency from three tests in ten years to one test in ten years. 
    For Type B and Type C tests, Option B allows plants to reduce 
    testing frequency based on the leak rate test history of each 
    component. In addition, Option B establishes controls to ensure 
    continued satisfactory performance of the affected penetrations 
    during the extended testing interval. To be consistent with the 
    requirements of Option B to 10 CFR 50, Appendix J, ComEd proposes to 
    include appropriate changes to the TSs that incorporate the 
    necessary revisions.
        Some of the proposed changes represent minor curtailments to 
    current TS requirements, but are based on the requirements specified 
    by Option B to 10 CFR 50, Appendix J. Any such changes are 
    consistent with the current plant safety analyses and have been 
    determined to represent sufficient requirements for the assurance of 
    the reliability of equipment assumed to operate in the safety 
    analyses, or provide continued assurance that specified parameters 
    associated with containment integrity remain within their acceptance 
    limits. The other proposed changes maintain consistency with those 
    requirements specified by Option B to 10 CFR 50, Appendix J and are 
    consistent with the current plant safety analyses. Implementation of 
    these changes will provide continued assurance that specified 
    parameters associated with containment integrity will remain within 
    their acceptance limits, and as such, will not significantly 
    increase the probability or consequences of a previously evaluated 
    accident.
        The associated systems affecting the leak rate integrity are not 
    assumed in any safety analyses to initiate any accident sequence; 
    therefore, the probability of occurrence of any accident previously 
    evaluated is not increased. In addition, the proposed changes to the 
    limiting conditions for operation and surveillance requirements for 
    such systems are consistent with the current 10 CFR 50, Appendix J, 
    requirements. The proposed changes maintain an equivalent level of 
    reliability and availability for all affected systems.
        Maintaining allowable leakage within the analyzed limit assumed 
    for the accident analyses does not adversely affect either the 
    onsite or offsite dose consequences. Furthermore, containment 
    leakage is not an accident initiator. As such, there is no adverse 
    impact on the probability of accident initiators. Thus, there is no 
    significant increase in the probability or occurrence of any 
    previously analyzed accident, or increase the consequences of any 
    previously analyzed accident.
        B. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Option B of 10 CFR 50, Appendix J, specifies, in part, that a 
    Type A test may be conducted at a periodic interval based on the 
    performance of the overall containment system. Type A tests measure 
    both the containment system overall integrated leakage rate at the 
    containment pressure boundary and system alignments assumed during a 
    large break loss-of-coolant accident (LOCA), and demonstrate the 
    capability of the primary containment to withstand an internal 
    pressure load. The acceptable leakage rates are specified in the 
    TSs. For Type B and C tests, intervals are proposed for 
    establishment based on the performance history of each component. 
    Acceptance criteria for each component are based upon demonstration 
    that the leakage rates at design basis pressure conditions for 
    applicable penetrations are within the limits specified in the TSs.
        The proposed changes reflect the requirements specified in the 
    amended 10 CFR 50, Appendix J, and are consistent with the current 
    plant safety analyses. Some minor curtailments of current TS 
    requirements are 
    
    [[Page 7548]]
    based on generic guidance or similarly approved provisions for other 
    plants. These changes do not involve revisions to the design of the 
    plant. Some of the changes may involve revision in the testing of 
    components at the plant; however, these are in accordance with the 
    current plant safety analyses and provide for appropriate testing or 
    surveillance that is consistent with Option B to 10 CFR 50, Appendix 
    J. The proposed changes will not introduce new failure mechanisms 
    beyond those already considered in the current plant safety 
    analyses.
        No new modes of operation are introduced by the proposed 
    changes. Surveillance requirements are changed to reflect 
    corresponding changes associated with Option B to 10 CFR 50, 
    Appendix J. The proposed changes maintain at least the present level 
    of operability of any such system that affects plant containment 
    integrity. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated. The associated systems that affect plant leak 
    rate integrity related to the proposed amendment are not assumed to 
    initiate any accident sequence. In addition, the proposed 
    surveillance requirements for any such affected systems are 
    consistent with the current requirements specified within the TSs 
    and are consistent with the requirements of Option B to 10 CFR 50, 
    Appendix J. The proposed surveillance requirements maintain an 
    equivalent level of reliability and availability of all affected 
    systems and, therefore, do not affect the consequences of any 
    previously evaluated accident. As such, the probability of systems 
    associated with leak rate test integrity failing to perform their 
    intended function is unaffected by the proposed limiting conditions 
    for operation and surveillance requirements.
        C. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The provisions specified in Option B to 10 CFR 50 Appendix J, 
    allows changes to Type A, B, and C test intervals based upon the 
    performance of past leak rate tests. The effect of extending 
    containment leak rate test intervals is a corresponding increase in 
    the likelihood of containment leakage. The degree to which intervals 
    can be extended has a direct impact on the potential effect on 
    existing plant safety margins and the public health and safety that 
    can occur due to an increased likelihood of containment leakage.
        Changing Type A, B, and C test intervals from those currently 
    provided in the TS to those provided for in 10 CFR 50, Appendix J, 
    Option B, slightly increases the risk associated with Type A, B, and 
    C specific accident sequences. Historical data suggest that 
    increasing the Type C test interval can slightly increase the 
    associated risk; however, this is compensated by the corresponding 
    risk reduction benefits associated with reduction in component 
    cycling, stress, and wear associated with increased test intervals. 
    In addition, when considering the total integrated risk, which 
    includes all analyzed accident sequences, the additional risk 
    associated with increasing test intervals is negligible.
        The proposed changes are consistent with those provisions 
    specified in Option B of 10 CFR 50, Appendix J, and are consistent 
    with current plant safety analyses. In addition, these proposed 
    changes do not involve revisions to the design of the plant. As 
    such, the proposed individual changes will maintain the same level 
    of reliability of the equipment associated with containment 
    integrity, assumed to operate in the plant safety analysis, or 
    provide continued assurance that specified parameters affecting 
    plant leak rate integrity, will remain within their acceptance 
    limits. Therefore, the proposed changes provide continued assurance 
    of the leakage integrity of the containment without adversely 
    affecting the public health and safety and, as such, will not 
    significantly reduce existing plant safety margins.
        The proposed changes are based on United States Nuclear 
    Regulatory Commission (USNRC) accepted provisions and maintain 
    necessary levels of system or component reliability affecting plant 
    containment integrity. The performance-based approach to leakage 
    rate testing concludes that the impact on public health and safety 
    due to revised testing intervals is negligible. The proposed changes 
    will not reduce the availability of systems associated with 
    containment integrity when they are required to mitigate accident 
    conditions; therefore, the proposed changes do not involve a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    
        Date of amendment requests: December 4, 19, 19, 20, 20, and 20, 
    1995.
        Description of amendment request: Each proposed amendment would 
    change the surveillance requirement frequency from the current once per 
    18-month interval to once per 24-month which is the proposed length of 
    a Haddam Neck refueling cycle. The changes pertain to the following 
    equipment:
        December 4, 1995, Reactivity control systems flow paths, rod 
    position indication system, and Rod drop time.
        December 19, 1995, Containment Air Recirculation System.
        December 19, 1995, Main steam line (MSL) Code Safety Valves self 
    actuation, auxiliary feedwater system, service water system, snubber 
    testing, feedwater isolation valve actuation, and primary auxiliary 
    building cleanup system.
        December 20, 1995, reactor coolant system (RCS) interlock, 
    containment sump, High Pressure Safety Injection Pump and Low Pressure 
    Safety Injection autostart and alignment, containment spray, and PH 
    control.
        December 20, 1995, Trip actuating devices and channel trips, 
    reactor trip system, reactor trip system instrumentation, and accident 
    monitoring instrumentation.
        December 20, 1995, RCS flow indicators, Loop stop valve interlock, 
    Pressurizer code safety valves, Emergency power supply for the 
    pressurizer heaters, Containment main sump and volume control tank 
    (VCT) level monitoring system, RCS pressure boundary valves, Low 
    temperature overpressure protection (LTOP) system, and RCS vent path.
        Basis for proposed no significant hazards consideration 
    determination: The Commission has made a proposed determination that 
    the amendment request involves no significant hazards consideration. 
    Under the Commission's regulations in 10 CFR 50.92, this means that 
    operation of the facility in accordance with the proposed amendment 
    would not (1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated; or (2) create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated; or (3) involve a significant reduction in a 
    margin of safety. As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
        1. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes to surveillance requirements of the Haddam 
    Neck Plant Technical Specifications extend the frequency for checking 
    the operability of the affected components/equipment. The proposal 
    would extend the frequency from at least once per 18 months to at least 
    once each refueling interval (i.e., nominal 24-months).
    
    [[Page 7549]]
    
        Changing the frequency of surveillance requirements from at least 
    once per 18 months to at least once each refueling interval does not 
    change the basis for the frequency. The frequency was chosen because of 
    the need to perform this verification under the conditions that apply 
    during a plant outage, and to avoid the potential of an unplanned 
    transient if the surveillance were conducted with the plant at power.
        The proposed changes do not alter the intent or method by which the 
    surveillance are conducted, do not involve any physical changes to the 
    plant, do not alter the way any structure, system, or component 
    functions, and do not modify the manner in which the plant is operated. 
    As such, the proposed changes in the frequency of surveillance 
    requirements will not degrade the ability of the equipment/components 
    to perform its safety function.
        Additional assurance of the operability of the components/equipment 
    is provided by additional surveillance requirements (e.g., monthly or 
    quarterly surveillance).
        Equipment performance over the last four operating cycles was 
    evaluated to determine the impact of extending the frequency of 
    surveillance requirements. This evaluation included a review of 
    surveillance results, preventive maintenance records, and the frequency 
    and type of corrective maintenance. It concluded that there is no 
    indication that the proposed extension could cause deterioration in the 
    condition or performance of any of the subject components.
        In addition to the substantive changes, there are format changes 
    which are merely editorial and because format changes produce no 
    physical change they do not influence the probability or consequences 
    of accidents.
        Since the proposed changes only affect the surveillance frequency 
    for safety systems that are used to mitigate accidents, the changes 
    cannot affect the probability of any previously analyzed accident. 
    While the proposed changes can lengthen the intervals between 
    surveillance, the increases in intervals has been evaluated and it is 
    concluded that there is no significant impact on the reliability or 
    availability of the safety system and consequently, there is no impact 
    on the consequences on any analyzed accident.
        2. The changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed changes to surveillance requirements of the Haddam 
    Neck Plant Technical Specifications extend the frequency for verifying 
    the operability of the affected components/equipment. The proposal 
    would extend the frequency from at least once per 18 months to at least 
    once each refueling interval (nominal 24 months).
        Changing the frequency of surveillance requirements from at least 
    once per 18 months to at least once each refueling interval does not 
    change the basis for the frequency. The frequency was chosen because of 
    the need to perform this verification under the conditions that apply 
    during a plant outage, and to avoid the potential of an unplanned 
    transient if the surveillance were conducted with the plant at power.
        In addition to the substantive changes, there are format changes 
    which are merely editorial and because format changes produce no 
    physical change they do not influence the probability of new or 
    different types of accidents.
        The proposed changes do not alter the intent or method by which the 
    surveillance are conducted, do not involve any physical changes to the 
    plant, do not alter the way any structure, system, or component 
    functions, and do not modify the manner in which the plant is operated. 
    As such, the proposed changes cannot create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The changes do not involve a significant reduction in a margin 
    of safety.
        The proposed changes to surveillance requirements of the Haddam 
    Neck Plant Technical Specifications extend the frequency for verifying 
    the operability of the components/equipment. The proposal would extend 
    the frequency from at least once per 18-months to at least once each 
    refueling interval (24-months).
        In addition to the substantive changes, there are format changes 
    which are merely editorial and because format changes produce no 
    physical change they do not influence the margin of safety.
        The proposed changes to surveillance frequency are still consistent 
    with the basis for the frequency, and the intent or method of 
    performing the surveillance is unchanged. Further, the current 
    inservice testing requirements and the previous history of reliability 
    of the system provides assurance that the changes will not affect the 
    reliability of the auxiliary feedwater system. Thus, it is concluded 
    that there is no impact on the margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County and Northeast Nuclear Energy Company, et al., 
    Docket Nos. 50-245, 50-336, and 50-423, Millstone Nuclear Power 
    Station, Units 1, 2, and 3, New London County, Connecticut
    
        Date of amendment request: June 6, 1995 (published August 2, 1995, 
    60 FR 39434), as supplemented November 22, 1995.
        Description of amendment request: The proposed amendments will 
    modify the size of the Plant Operations Review Committee (PORC) which 
    will collectively have the experience and expertise in various areas of 
    plant operation, and will clarify the composition of the Site 
    Operations Review Committee (SORC).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
        . . . These proposed changes do not involve an SHC because the 
    changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The plant operations review committee (PORC) is an oversight 
    group and helps to ensure that the units are operated in a safe 
    manner. To accomplish this the PORCs provide their recommendations 
    on the safety related activities to the Vice President--Haddam Neck 
    Plant for Haddam Neck and to the respective Nuclear Unit Directors 
    for Millstone. Each Millstone Unit has its own PORC. It is proposed 
    that the members of the Millstone PORCs be selected by the 
    respective Nuclear Unit Director based on their knowledge and 
    expertise in specific key plant functions. The Millstone Station has 
    one site operations review committee (SORC). The SORC is also an 
    oversight group whose charter is to advise the Senior Vice 
    President--Millstone Station on all matters related to nuclear 
    safety at the Millstone site. The Haddam Neck Plant, being a single 
    unit site, has one PORC, which advises the Vice President--Haddam 
    Neck Plant. The members of the Haddam Neck Plant PORC will be 
    selected by the Vice President--Haddam Neck Plant based on their 
    knowledge and expertise in specific key 
    
    [[Page 7550]]
    plant functions. The PORC and SORC add to the defense-in-depth concept 
    provided by the design, operation, maintenance, and quality 
    oversight by promoting excellence through the conduct of their 
    affairs and by maintaining a diligent watch over their 
    responsibilities.
        These administrative changes will revise the composition section 
    of the technical specifications for the PORC members. Millstone Unit 
    individuals will be appointed by the Nuclear Unit Directors if the 
    individual meets one or more of the following areas of expertise: 
    Plant Operations, Engineering, Reactor Engineering, Maintenance, 
    Instrumentation and Controls, Health Physics, Chemistry, Work 
    Planning and Control, and Quality Services. The Haddam Neck Plant, 
    due to its broader scope of review also include an individual 
    experienced in Security and specific expertise in Electrical 
    Maintenance and Mechanical Maintenance. The individuals who will 
    serve on PORC shall continue to meet the criteria of ANSI N18.1-1971 
    along with the qualification requirements contained in the technical 
    specifications. This approach is consistent with the standard 
    technical specifications and NUREG 0800, Section 13.4. For SORC at 
    the Millstone Station, the method of identifying who shall serve as 
    Vice Chairperson has been modified for clarity. Finally, the 
    individual who shall represent Quality and Assessment Services shall 
    be modified to allow a qualified member of Quality and Assessment 
    Services to serve on SORC.
        The remaining portions of the technical specifications related 
    to PORC and SORC are not being revised.
        These modifications broaden the unit committee participation and 
    reflect current organizational positions and will not increase the 
    probability of occurrence or the consequences of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed administrative enhancements to the composition of 
    the PORC and Millstone Station SORC will not affect the way in which 
    the units are physically operated. These administrative changes to 
    PORC and SORC continue to meet the guidelines of ANSI N18.7-1976. 
    The modifications to PORC and SORC continue to allow these groups to 
    provide a thorough review of activities at the units.
        The proposed modification does not impact any initiating events, 
    and therefore, cannot create the possibility of any new or different 
    kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        These proposed administrative changes will not impact the margin 
    of safety provided by PORC and SORC. The PORC and SORC will continue 
    to be staffed by qualified individuals experienced in the operation 
    of the plants. These administrative changes will modify how the 
    composition of the PORC and SORC members are presented in the 
    technical specifications, but will not adversely impact their 
    ability to review and comment on operations at the units.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street Middletown, Connecticut 06457, for the Haddam Neck Plant, and 
    the Learning Resources Center, Three Rivers Community-Technical 
    College, 574 New London Turnpike, Norwich, CT 06360, for Millstone 1, 
    2, and 3.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: November 22, 1995 (NRC-95-0124).
        Description of amendment request: The proposed amendment would 
    modify the allowed out-of-service time for one onsite alternating 
    current (ac) electrical power division from 72 hours to 7 days. The 
    proposed amendment would also eliminate accelerated testing and special 
    reports as a result of diesel generator surveillance failures in 
    accordance with Generic Letter 94-01, ``Removal of Accelerated Testing 
    and Special Reporting Requirements for Emergency Diesel Generators,'' 
    dated May 31, 1994.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident. Changing the out-of-
    service time, surveillance frequency and reporting requirements for 
    emergency diesel generators (EDGs) will not affect the initiation of 
    an accident, since EDGs are not associated with any accident 
    initiation mechanism. The proposed changes will not impact the plant 
    design or method of EDG operation. The increased out-of-service time 
    has been evaluated to have only a small impact on plant risk. 
    Performing the EDG inspections during plant operations will decrease 
    plant risk during plant outages. Deleting the accelerated testing 
    provisions will not affect the consequences of an accident since the 
    implementation of a maintenance and monitoring program for EDGs 
    consistent with the provisions of the maintenance rule will assure 
    EDG performance as discussed in Generic Letter 94-01. Deleting 
    reporting requirements has no impact on consequences of an accident 
    since reporting has no accident effect. Based on the amount of 
    electrical system redundancy, the small increase in plant risk 
    during operations and the decrease in plant risk during outages, 
    this change will not result in a significant increase in the 
    probability or consequences of an accident.
        2. The proposed changes do not create the possibility of a new 
    or different accident from any previously evaluated. The proposed 
    changes do not modify the plant design or method of diesel 
    operation. Therefore, no new accident initiator is introduced, nor 
    is a new type of failure created. For these reasons, no new or 
    different type of accident is created by these changes.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety. Since implementation of a maintenance program 
    for the EDGs consistent with the Maintenance Rule will ensure that 
    high EDG performance standards are maintained, the accelerated 
    testing schedule is not needed to maintain the margin of safety. 
    Deleting reporting requirements has no impact on safety or margin of 
    safety. Increasing the allowed out-of-service time for one division 
    of onsite AC power will slightly increase EDG unavailability during 
    plant operation. However, this change does not impact the redundancy 
    of offsite power supplies, the allowed out-of-service time if both 
    divisions are inoperable, or the ability to cope with a station 
    blackout event. This request also does not change the Action 
    statement for AC electrical power systems required when the plant is 
    shutdown. The increase in core damage frequency was assessed to be 
    small by an evaluation using the plant PSA [probabilistic safety 
    assessment] for the operating condition. Enabling the diesel 
    generator inspections to be performed on-line will improve safety 
    while shutdown by reducing EDG out-of-service time during outages. 
    For these reasons, the proposed changes do not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Project Director: John N. Hannon. 
        
    [[Page 7551]]
    
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: December 21, 1995 (NRC-95-0133).
        Description of amendment request: The proposed amendment would 
    implement Option B of the recently revised 10 CFR Part 50 Appendix J in 
    a manner consistent with Regulatory Guide 1.163, ``Performance-Based 
    Containment Leak Test Program,'' and industry guidance contained in NEI 
    94-01, Revision 0, ``Industry Guideline for Implementing Performance-
    Based Option of 10 CFR 50, Appendix J,'' with the exception of 
    previously approved exemptions which the licensee wishes to remain in 
    effect. The previously approved exemptions are for reduced pressure for 
    testing MSIVs [main steam isolation valves] and testing of LPCI [low 
    pressure coolant injection] isolation valves in accordance with 
    Technical Specification (TS) 4.4.3.2.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. This request does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change implements the new Option B of 10 CFR Part 
    50 Appendix J on performance-based containment leakage testing. The 
    proposed change does not involve a change to the plant design or 
    operation. As a result, the proposed change does not affect any 
    parameters or conditions that contribute to the initiation of any 
    accidents previously evaluated. Thus, the proposed change cannot 
    increase the probability of any accident previously evaluated.
        The proposed change potentially affects the leak-tight integrity 
    of the containment structure designed to mitigate the consequences 
    of a loss-of-coolant accident (LOCA). The function of the 
    containment is to maintain functional integrity during and following 
    the peak transient pressures and temperatures which result from any 
    loss-of-coolant accident (LOCA). The containment is designed to 
    limit fission product leakage following the design basis LOCA. 
    Because the proposed change does not alter the plant design, only 
    the frequency of measuring Type A, B, and C leakage, the proposed 
    change does not directly result in an increase in containment 
    leakage. However, decreasing the test frequency can increase the 
    probability that an increase in containment leakage could go 
    undetected for an extended period of time. Test intervals will be 
    established based on the performance history of components being 
    tested. The risk resulting from the proposed changes is 
    characterized as follows, based primarily on the results contained 
    in NUREG-1493 [''Performance-Based Containment Leakage Test 
    Program''], the principal Technical Support Document used by the NRC 
    as the basis for the Appendix J final rule (Reference 9 [of 
    application]) and the NRC's Final Regulatory Impact Analysis as 
    contained in SECY-95-181 [Final Regulatory Impact Analysis, 
    Performance-Based Containment Leakage-Test Program (Attachment 2 to 
    NRC Rulemaking Issue Affirmation, SECY-95-181 dated July 17, 1995, 
    Final Amendment to 10 CFR 50, Appendix J, ``Containment Leakage 
    Testing,'' to Adopt Performance-Oriented and Risk-Based Approaches)] 
    (Reference 10 [of application]):
    
    Type A Testing
    
        NUREG-1493 found that the effect of containment leakage on 
    overall accident risk is minimal since risk is dominated by accident 
    sequences that result in failure or bypass of the containment.
        Industry wide, ILRTs [integrated leak rate tests] have only 
    found a small fraction of the leaks that exceed current acceptance 
    criteria. Only three percent of all leaks are detectable only by 
    ILRTs, and therefore, by extending the Type A testing intervals, 
    only three percent of all leaks have a potential for remaining 
    undetected for longer periods of time. In addition, when leakage has 
    been detected by ILRTs, the leakage rate has been only marginally 
    above existing requirements. The Fermi Type A testing confirms the 
    industry-wide experience that a majority of the leakage experienced 
    during Type A testing is through components tested by Type B and C 
    tests.
        NUREG-1493 found that these observations, together with the 
    insensitivity of reactor accident risk to the containment leakage 
    rate, show that increasing the Type A leakage test intervals would 
    have a minimal impact on public risk.
    
    Type B and C Testing
    
        NUREG-1493 found that while Type B and C tests can identify the 
    vast majority (greater than 95 percent) of all potential leakage 
    paths, performance-based alternatives to current local leakage-
    testing requirements are feasible without significant risk impacts. 
    The risk model used in NUREG-1493 suggests that the number of 
    components tested would be reduced by about 60 percent with less 
    than a three-fold increase in the incremental risk due to 
    containment leakage. Since, under existing requirements, leakage 
    contributes less than 0.1 percent of overall accident risk, the 
    overall impact is very small. In addition, the NRC's Final 
    Regulatory Impact Analysis concluded that while the extended testing 
    intervals for Type B and C tests led to minor increases in potential 
    offsite dose consequences, the beneficial expected decrease in 
    onsite (LLRT [local leak rate testing] & ILRT worker) dose exceeds 
    (by at least an order of magnitude) the potential off-site dose 
    consequences.
        The editorial change to the bases has no impact on the 
    probability or consequence of an accident since it is strictly a 
    correction to achieve consistency between the bases and the 
    specifications.
        Based on the above, DECO [the licensee] has concluded that the 
    proposed change will not result in a significant increase in the 
    probability or consequences of any accident previously evaluated.
        2. The request does not create the possibility of occurrence of 
    a new or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that could contribute to 
    initiation of any accidents. This change involves the reduction of 
    Type A, B, and C test frequency. Except for the method of defining 
    the test frequency, the methods for performing the actual tests are 
    not changed. No new accident modes are created by extending the 
    testing intervals. No safety-related equipment or safety functions 
    are altered as a result of this change. Extending the test frequency 
    has no influence on, nor does it contribute to, the possibility of a 
    new or different kind of accident or malfunction from those 
    previously analyzed.
        The editorial change to the bases has no effect on any kind of 
    accident since it is strictly a correction to achieve consistency 
    between the bases and the specifications.
        Based on the above, DECO has concluded that the proposed change 
    will not create the possibility [of] a new or different kind of 
    accident previously evaluated.
        3. The request does not involve a significant reduction in a 
    margin to safety.
        The proposed change only affects the frequency of Type A, B, and 
    C testing. Except for the method of defining the test frequency, the 
    methods for performing the actual tests are not changed. However, 
    the proposed change can increase the probability that an increase in 
    leakage could go undetected for an extended period of time. NUREG-
    1493 has determined that, under several different accident 
    scenarios, the increased risk of radioactivity release from 
    containment is negligible with the implementation of these proposed 
    changes.
        The margin of safety that has the potential of being impacted by 
    the proposed change involves the offsite dose consequences of 
    postulated accidents which are directly related to containment 
    leakage rate. The containment isolation system is designed to limit 
    leakage to La, which is defined by the Fermi 2 Technical 
    Specifications to be 0.5 percent by weight of the containment air 
    per 24 hours at 56.5 psig (Pa). The limitation on containment 
    leakage rate is designed to ensure that total leakage volume will 
    not exceed the value assumed in the accident analyses at the peak 
    accident pressure (Pa). The margin to safety for the offsite 
    dose consequences of postulated accidents directly related to the 
    containment leakage rate is maintained by meeting the 1.0 La 
    acceptance criteria. The La value is not being modified by this 
    proposed Technical Specification change.
        Except for the method of defining the test frequency, no change 
    in the method of testing is being proposed. The Type B and C tests 
    will continue to be done at full pressure (Pa) or greater with 
    the exception of the Main Steam Isolation Valves, which have an 
    approved exemption. Other programs are in 
    
    [[Page 7552]]
    place to ensure that proper maintenance and repairs are performed 
    during the service life of the primary containment and systems and 
    components penetrating the primary containment.
        The editorial change to the bases has no effect on the margin of 
    safety since it is strictly an editorial change to achieve 
    consistency between the bases and the specifications.
        As a result, DECO has concluded that the proposed change will 
    not result in a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Project Director: John N. Hannon.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    No. 50-498, South Texas Project, Unit 1, Matagorda County, Texas
    
        Date of amendment request: January 22, 1996.
        Description of amendment request: The proposed amendment would 
    modify the steam generator tube plugging criteria in Technical 
    Specification 3/4.4.5, Steam Generators, and the allowable leakage in 
    Technical Specification 3/4.4.6.2, Operational Leakage, and the 
    associated Bases. The amendment would allow the implementation of 
    alternate steam generator tube plugging criteria for the tube support 
    plate (TSP)/tube intersections for Unit 1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
    
    Structural Considerations
    
        Industry testing of model boiler and operating plant tube 
    specimens for free span tubing at room temperature conditions show 
    typical burst pressures in excess of 5000 psi for indications of 
    outer diameter stress corrosion cracking with voltage measurements 
    at or below the structural limit of 4.0 volts. One model boiler 
    specimen with a voltage amplitude of 19 volts also exhibited a burst 
    pressure greater than 5000 psi. Burst testing performed on one 
    intersection pulled from STP Unit 1 in 1993 with a 0.51 volt 
    indication yielded a measured burst pressure of 8900 psi at room 
    temperature. Burst testing performed on another intersection pulled 
    from STP Unit 1 in 1995 with a 0.48 volt indication yielded a 
    measured burst pressure of 9950 psi at room temperature.
        The projected end-of-cycle (EOC) voltage compares favorably with 
    the 4.7 volt structural limit considering the EPRI [Electric Power 
    Research Institute] voltage growth rate for indications at STP. 
    Using the methodology of the NRC Generic Letter 95-05, the 
    structural limit is reduced by allowances for uncertainty and growth 
    to develop a beginning-of-cycle (BOC) repair limit which should 
    preclude EOC indications from growing in excess of the structural 
    limit. The non-destructive examination (NDE) uncertainty to be 
    applied per EPRI is approximately 20 percent. The EPRI recommended 
    growth allowance of 30 percent/EFPY [effective full power year] is 
    also to be applied. This growth value is conservative for STP Unit 1 
    based on previous inspection history. By adding NDE uncertainty 
    allowances and a crack growth allowance to the repair limit, the 
    structural limit can be validated. Therefore, the maximum allowable 
    BOC repair limit (RL) based on the structural limit of 4.7 volts can 
    be represented as:
    
    RL + (0.20 x RL) + (0.45* x RL) = 4.7 volts, which yields RL of 2.85 
    volts.
    
        * The 30% growth rate for 1 EFPY was scaled up to the cycle 
    length used at South Texas.
    
        This repair limit (2.85 volts) reasonably could be applied for 
    APC [alternate plugging criteria] implementation to repair bobbin 
    indications greater than the 1.0 volt criterion specified by NRC 
    Generic Letter 95-05 and is independent of RPC [rotating pancake 
    coil-probe] confirmation of the indications. STP has chosen to use a 
    steam generator tube upper repair limit of 2.85 volts to assess tube 
    integrity for those bobbin indications which are above 1.0 volt but 
    do not have confirming RPC calls. This 2.85 volt upper limit for 
    non-confirmed RPC calls is consistent with the NRC Generic Letter 
    95-05. Since the upper bound for repair of non-confirmed RPC is 
    limited to a value far less than the structural limit associated 
    with a full alternate criteria, the establishment of the repair 
    limits are determined to be reasonable and conservative with respect 
    to the industry pulled tube data base used.
    
    Leakage Considerations
    
        As part of the implementation of APC, the distribution of EOC 
    cracking indications at the TSP intersections has been used to 
    calculate the primary-to-secondary leakage which is bounded by the 
    maximum leakage required to remain within applicable dose limits. 
    This limit was calculated using the Technical Specification RCS 
    [reactor coolant system] Iodine-131 transient spiking values 
    consistent with NUREG-0800. Application of the APC criteria requires 
    the projection of postulated MSLB [main steam line break] leakage 
    based on the projected EOC voltage distribution for the beginning of 
    cycle. Projected EOC voltage distribution is developed using the 
    most recent EOC eddy current results and a voltage measurement 
    uncertainty. Draft NUREG-1477 requires that all indications to which 
    APC is applied must be included in the leakage projection.
        The projected MSLB leakage rate calculation methodology 
    prescribed in EPRI TR-100407 will be used to calculate the EOC 
    leakage. A Monte Carlo approach will be used to determine the EOC 
    leakage, accounting for all of the ECT [eddy current testing] 
    uncertainties, voltage growth, and an assumed probability of 
    detection (POD) of 0.6 for a 1.0 volt repair limit. The fitted 
    logarithmic function probability of leakage correlation will be used 
    to establish the STP MSLB leak rate used for comparison with a 
    bounding allowable leak rate in the faulted loop which would result 
    in radiological consequences which are within applicable dose 
    limits. Due to the relatively low voltage levels of indications at 
    STP and low voltage growth rates, it is expected that the actual 
    calculated leakage values will be far less than this limit.
        Therefore, implementation of APC does not adversely affect steam 
    generator tube integrity and implementation will be shown to result 
    in acceptable dose consequences. The proposed amendment does not 
    result in any increase in the probability or consequences of an 
    accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Implementation of the proposed steam generator tube alternate 
    plugging criteria for ODSCC [outer diameter stress corrosion 
    cracking] at the TSP intersections does not introduce any 
    significant changes to the plant design basis. Use of the criteria 
    does not provide a mechanism which could result in an accident 
    outside of the region of the TSP elevations since no ODSCC has been 
    identified outside the thickness of the TSPs. It is therefore 
    expected that for all plant conditions, neither a single or multiple 
    tube rupture event would occur in a steam generator where APC has 
    been applied.
        Specifically, STP will implement, for Unit 1, a maximum leakage 
    rate of 150 gpd [gallons per day] per steam generator (SG) to help 
    preclude the potential for excessive leakage during all plant 
    conditions. The current technical specification limits on primary-
    to-secondary leakage at operating conditions are 1 gpm [gallon per 
    minute] for all steam generators or 500 gpd for any one SG. The RG 
    [Regulatory Guide] 1.121 criterion for establishing operational 
    leakage rate limits governing plant shutdown is based upon leak-
    before-break (LBB) considerations to detect a free span crack before 
    potential tube rupture as a result of faulted plant conditions. The 
    150 gpd limit is intended to provide for leakage detection and plant 
    shutdown in the event of an unexpected crack propagation resulting 
    in excessive leakage. RG 1.121 acceptance criteria for establishing 
    operating leakage limits are 
    
    [[Page 7553]]
    based on LBB considerations such that plant shutdown is initiated if 
    the permissible crack is exceeded.
        The predicted EOC leakage for STP is based on the calculated 
    growth rate and does not take credit for the TSP proximity during 
    normal operation. Thus, the 150 gpd limit provides for plant 
    shutdown prior to reaching critical crack lengths. Additionally, 
    this leak-before-break evaluation assumes that the entire crevice 
    area is uncovered during the secondary side blowdown of a MSLB. 
    Typically, it is expected for the vast majority of intersections 
    that only partial uncovery will occur. Thus, the proximity of the 
    TSP will enhance the burst capacity of the tube.
        Steam generator tube integrity is continually maintained through 
    inservice inspection and primary-to-secondary leakage monitoring. 
    Any tubes falling outside the APC repair limits are removed from 
    service. Therefore, the possibility of a new or different kind of 
    accident from any accident previously developed is not created.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The use of the voltage based bobbin probe for dispositioning 
    ODSCC degraded tubes within TSP intersections by APC is demonstrated 
    to maintain steam generator tube integrity in accordance with the 
    requirements of RG 1.121. RG 1.121 describes a method acceptable to 
    the NRC staff for meeting GDCs [General Design Criterion] 14, 15, 
    31, and 32 by reducing the probability or the consequences of steam 
    generator tube rupture. This is accomplished by determining the 
    limiting conditions of degradation of steam generator tubing, as 
    established by inservice inspection, for which tubes with 
    unacceptable cracking are removed from service. Upon implementation 
    of the criteria, even under the worst case conditions, the 
    occurrence of ODSCC at the TSP elevation is not expected to lead to 
    a steam generator tube rupture event during normal or faulted plant 
    conditions. The EOC distribution of crack indications at the TSP 
    elevations will be confirmed to result in acceptable primary-to-
    secondary leakage during all plant conditions and that radiological 
    consequences are not adversely impacted.
        In addressing the combined effects of loss of coolant accident 
    (LOCA) and safe shutdown earthquake (SSE) on the steam generator 
    component (as required by GDC 2), it has been determined that tube 
    collapse may occur in the steam generators at some plants. This is 
    the case at STP as the TSP may become deformed as a result of 
    lateral loads at the wedge supports at the periphery of the plate 
    due to the combined effects of the LOCA rarefaction wave and SSE 
    loadings. The resulting secondary-to-primary pressure differential 
    on the deformed tubes may cause some of the tube to collapse.
        There are two concerns associated with steam generator tube 
    collapse. First, the collapse of steam generator tubing reduces the 
    RCS flow area through the tubes. The reduction in flow area 
    increases the resistance to flow of steam from the core during a 
    LOCA which, in turn, may potentially increase peak clad temperature 
    (PCT). Second, there is a potential that through wall cracks in 
    tubes could sufficiently enlarge during tube deformation or 
    collapse, causing sufficient in-leakage of secondary water back to 
    the core which dilutes the poisoning effect of boron injection from 
    the emergency cooling system. Again, an increase in core PCT may 
    result.
        Consequently, since the LBB methodology is applicable to the STP 
    reactor coolant loop piping, the probability of breaks in the 
    primary loop piping is sufficiently low that they need not be 
    considered in the structural design of the plant. The analysis 
    identified tubes located adjacent to wedge regions that are subject 
    to potential collapse during combined LOCA and SSE. These tubes will 
    be excluded from application of APC. Thus, existing tube integrity 
    requirements apply to these tubes and the margin of safety is not 
    reduced.
        Implementation practices using the bobbin probe voltage based 
    tube plugging criteria bounds RG 1.83 considerations by:
        (1) Using enhanced eddy current inspection guidelines consistent 
    with those used by EPRI in developing the correlations. This 
    provides consistency in voltage normalization,
        (2) Performing a 100 percent bobbin coil inspection for all hot 
    leg tube support plate intersections and all cold leg intersections 
    down to the lowest cold leg tube support plate with outer diameter 
    stress corrosion cracking (ODSCC) indications. The determination of 
    the tube support plate intersections having ODSCC indications shall 
    be based on the performance of at least a 20% random sampling of 
    tubes inspected over their full length, and
        (3) Incorporating RPC inspection for all tubes with larger 
    indications left in service. This further establishes the principal 
    degradation morphology as ODSCC.
        Implementation of APC at TSP intersections will decrease the 
    number of tubes which must be repaired. Since the installation of 
    tube plugs (to remove ODSCC degraded tubes from service) reduces the 
    RCS flow margin, APC implementation will help preserve the margin of 
    flow that would otherwise be reduced.
        For each cycle the projected EOC primary-to-secondary leak rate 
    allowed is bounded by a leak rate which limits the radiological 
    consequences of a EOC MSLB to within applicable dose limits. 
    Therefore, this change does not involve a significant reduction in 
    the margin to safety.
        It is therefore concluded that the proposed license amendment 
    request does not result in a significant reduction in the margin of 
    safety as defined in the plant Final Safety Analysis Report or 
    Technical Specifications.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869.
        NRC Project Director: William D. Beckner.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    No. 50-498, South Texas Project, Unit 1, Matagorda County, Texas
    
        Date of amendment request: January 22, 1996.
        Description of amendment request: The proposed amendment would 
    modify the steam generator tube plugging criteria in Technical 
    Specification 3/4.4.5, Steam Generators, and the associated Bases, to 
    allow the implementation of alternate steam generator tube plugging 
    criteria for the tube-to-tubesheet joints (known in the industry as F*) 
    for Unit 1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes to the Steam Generator section of Technical 
    Specifications do not affect any accident initiators or precursors 
    and do not alter the design assumptions for the systems or 
    components used to mitigate the consequences of an accident. The 
    requirements approved by the NRC will not be reduced by this 
    request. Since F* utilizes the ``as rolled'' tube configuration that 
    exists as part of the original steam generator design, all of the 
    design and operating characteristics of the steam generator and 
    connected systems are preserved. The F* joint has been analyzed and 
    tested for design, operating and faulted condition loadings in 
    accordance with Regulatory Guide 1.121 safety factors. At worst 
    case, a tube leak would occur with the result being a primary to 
    secondary leak.
        Should a tube leak occur, the impact is bounded by the ruptured 
    tube evaluation submitted by STP for the Unit 1 operating license. 
    No new or unreviewed accident conditions are created by the use of 
    F* criteria. The potential for a tube rupture is not increased from 
    the original submittal, thus there is no impact on accidents 
    evaluated as the design basis. Therefore use of the F* criteria will 
    not increase the probability of occurrence of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. 
    
    [[Page 7554]]
    
        The use of the proposed F* alternate plugging criteria will not 
    introduce significant or adverse changes to the plant design basis. 
    The failure of a tube which remained unplugged in accordance with 
    the F* criteria would result in a tube leak, which is a previously 
    analyzed condition. Since this leak would occur below the secondary 
    face of the tubesheet, its leak rate would be limited by the tube-
    to-tubesheet interface. Qualification testing and previous 
    experience indicates that normal and faulted leakage would be well 
    below the technical specification limits creating no threat 
    associated with tube rupture type leakages. This conclusion is 
    consistent with previous F* programs approved and used at other 
    operating plants.
        However, in the unlikely event the failed tube severed 
    completely at a point below the F* region, the remaining F* joint 
    would retain engagement in the tubesheet due to its length of 
    expanded contact within the tubesheet bore, preventing any 
    interaction with neighboring tubes. If the tube severs at a point 
    above the F* region, then it is covered by the tube rupture event as 
    a part of the UFSAR [Updated Final Safety Analysis Report]. Thus, 
    the possibility of a new or different type of accident from any 
    accident previously evaluated is not created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Based on previous responses (above), the protective boundaries 
    of the steam generator are preserved. A tube with degradation can be 
    kept in service through F* criteria which provided an un-degraded 
    expanded interface with the tubesheet and which satisfies all of the 
    necessary structural and leakage requirements in accordance with 
    Regulatory Guide 1.121 and the Technical Specifications. Since the 
    joint is constrained within the tubesheet bore there is no 
    additional risk associated with tube rupture. Since the UFSAR 
    analyzed accident scenarios remain bounding, the use of an F* 
    criteria does not reduce the margin of safety.
        Thus, these changes do not involve a significant reduction in 
    the margin of safety. Therefore, based on the above evaluation, STP 
    has concluded that these changes do not involve any significant 
    hazards considerations.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869
        NRC Project Director: William D. Beckner.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: January 12, 1996 (AEP:NRC:1233).
        Description of amendment requests: The proposed amendments would 
    modify technical specification section 4.4.11 to eliminate the 
    surveillance requirement (SR) demonstrating operability of the 
    emergency power supply for the pressurizer power-operated relief valves 
    (PORVs) and block valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Per 10 CFR 50.92, a proposed change does not involve significant 
    hazards consideration if the change does not:
        1. involve a significant increase in the probability or 
    consequence of an accident previously evaluated,
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. involve a significant reduction in a margin of safety.
    
    Criterion 1
    
        The proposed change is consistent with NUREG-1431 [Standard 
    Technical Specifications Westinghouse Plants]. Due to the high 
    reliability and continued testing of the Class 1E power supply, we 
    conclude that the elimination of the SR will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
    
    Criterion 2
    
        The proposed change does not involve the addition of any new 
    plant operation or procedures, and the elimination of the SR is 
    consistent with NUREG-1431. For these reasons, we believe that the 
    proposed change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
    
    Criterion 3
    
        The proposed change is consistent with NUREG-1431, and it does 
    not affect the acceptance criteria of any of the other PORV and 
    block valve tests currently performed. For these reasons, we believe 
    that the proposed amendment will not involve a significant reduction 
    in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and the 
    applicable Bases of the Standard Technical Specifications Westinghouse 
    Plants. The Bases for the applicable surveillance, 3.4.11.4, states 
    ``This Surveillance is not required for plants with permanent 1E power 
    supplies to the valves.'' Based on this review, it appears that the 
    three standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC 
    staff proposes to determine that the amendment requests involve no 
    significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London, 
    Connecticut
    
        Date of amendment request: January 22, 1996.
        Description of amendment request: The proposed change relocates the 
    containment isolation valve (CIV) list, Table 3.6-2, from the Technical 
    Specifications to the Technical Requirements Manual (TRM). This change 
    affects Technical Specifications Sections 1.8.1a, 4.6.1.1a, 3.6.3.1, 
    4.6.3.1.1 and 4.6.3.1.2, and the Basis Section 3/4.6.3. A note at the 
    bottom of Table 3.6-2 regarding the CIVs that are subject to 
    administrative control is retained in the Technical Specifications by 
    relocating it to Sections 1.8.1a and 4.6.1.1a. This change is being 
    performed in accordance with Generic Letter 91-08, which provides 
    guidance for removal of component lists from the Technical 
    Specifications.
        Additionally, a change to provide relief in the surveillance 
    requirement in Section 4.6.1.1a is included. The change allows valves, 
    blind flanges, and deactivated automatic valves located inside the 
    containment and are locked, sealed, or otherwise secured in the closed 
    position to be verified closed during each cold shutdown but not more 
    often than once per 92 days. The current requirements check the valve 
    position once per 31 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
        Pursuant to 10CFR50.92, Northeast Nuclear Energy Company (NNECO) 
    has reviewed the proposed changes. NNECO concludes that these 
    changes do not involve a significant hazards consideration (SHC) 
    since the proposed changes satisfy the criteria in 10CFR50.92(c). 
    That is, the proposed changes do not: 
    
    [[Page 7555]]
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to remove the Containment Isolation Valve 
    (CIV) list from the Technical Specifications will not result in any 
    hardware or operating changes. The proposed change is based upon NRC 
    Generic Letter (GL) 91-08 and merely removes the CIV table and all 
    references to the table from the technical specifications without 
    affecting the operability requirements of any of the listed valves. 
    The technical specifications will continue to require the CIVs to be 
    operable. Limiting Condition for Operation and surveillance 
    requirements for the valves will also remain in the technical 
    specifications. The CIV table will be relocated to the Millstone 
    Unit No. 2 Technical Requirements Manual (TRM) which is controlled 
    in accordance with 10CFR50.59.
        This change is administrative in nature and does not involve an 
    increase in the probability or consequence of an accident previously 
    evaluated. Furthermore, the proposed change does not alter the 
    design, function, or operation of the valves involved, and therefore 
    does not affect the probability or consequences of any previously 
    evaluated accident.
        The change to Section 4.6.1.1a that reduces the surveillance 
    requirement for valves, blind flanges, and deactivated automatic 
    valves located inside the containment provides consistency with 
    NUREG-1432, ``Standard Technical Specifications for Combustion 
    Engineering Plants'' as well as the Technical Specifications of 
    Millstone Unit No. 3, Haddam Neck Plant, and Seabrook. The 
    probability or consequences of any previously evaluated accidents 
    are not affected.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The change to relocate the CIV list from the technical 
    specifications to the TRM will not impose any different operational 
    or surveillance requirements, nor will the change remove any such 
    requirements. Adequate control of information will be maintained. 
    Furthermore, as stated above, the proposed change does not alter the 
    design, function, or operation of the valves involved, and therefore 
    no new accident scenarios are created.
        The change to Section 4.6.1.1a that reduces the surveillance 
    requirement for valves, blind flanges, and deactivated automatic 
    valves located inside the containment does not alter the design, 
    function, or operation of the valves involved, and therefore no new 
    accident scenarios are created.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes will not reduce the margin of safety since 
    it has no impact on any safety analysis assumption. The proposed 
    changes do not decrease the scope of equipment currently required to 
    be operable or subject to surveillance testing, nor does the 
    proposed change affect any instrument setpoints or equipment safety 
    functions.
        The relocation of the valve list is consistent with the guidance 
    provided in GL 91-08. The change to the surveillance interval is 
    consistent with NUREG-1432, ``Standard Technical Specifications for 
    Combustion Engineering Plants'' as well as the Technical 
    Specifications of Millstone Unit No. 3, Haddam Neck Plant, and 
    Seabrook. The intent of the technical specification will be met 
    since the change will not alter function or operability requirements 
    for any CIV.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: January 17, 1996.
        Description of amendment request: The amendment request would 
    delete a license requirement to submit responses to and to implement 
    requirements of Generic Letter 83-28, because the requirement has been 
    completed. Generic Letter 83-28 pertains to the Salem anticipated 
    transient without scram (ATWS) event.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        . . . The proposed change does not involve an SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        NNECO's proposal to delete License Condition 2.C(4) is an 
    administrative change. The NRC Staff has accepted Millstone Unit No. 
    3's responses regarding the actions required by GL 83-28, thus, the 
    license condition has been met and is no longer necessary. The 
    proposed change does not affect the configuration, operation, or 
    performance of any system, structure, or component. Additionally, 
    the limiting conditions for operation, limiting safety system 
    settings, and safety limits specified in the Millstone Unit No. 3 
    Technical Specifications are unchanged. Therefore, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The NRC Staff has accepted Millstone Unit No. 3's responses 
    regarding the actions required by GL 83-28, thus, the license 
    condition has been met and is no longer necessary. The proposed 
    change to delete License Condition 2.C(4) does not affect the 
    configuration, operation, or performance of any system, structure, 
    or component. Additionally, the limiting conditions for operation, 
    limiting safety system settings, and safety limits specified in the 
    Millstone Unit No. 3 Technical Specifications are unchanged. 
    Therefore, this proposed change cannot create the possibility of a 
    new or different kind of accident from any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        The NRC Staff has accepted Millstone Unit No. 3's responses 
    regarding the actions required by GL 83-28, thus, the license 
    condition has been met and is no longer necessary. The proposed 
    change to delete License Condition 2.C(4) does not affect the 
    configuration, operation, or performance of any system, structure, 
    or component. Additionally, the limiting conditions for operation, 
    limiting safety system settings, and safety limits specified in the 
    Millstone Unit No. 3 Technical Specifications are unchanged. 
    Therefore, this proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of amendment request: December 22, 1995.
        Description of amendment request: The proposed changes will revise 
    Limerick Generating Station, Units 1 and 2, Technical Specification 
    3.6.1.8 ``Drywell and Suppression Chamber Purge System,'' increasing 
    the Drywell and Suppression Chamber Purge System operating time limit 
    from 90 hours each 365 days to 180 hours each 365 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the 
    
    [[Page 7556]]
    issue of no significant hazards consideration, which is presented 
    below:
    
        1. The proposed Technical Specification [TS] changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        These TS changes do not increase the probability of occurrence 
    of an accident previously evaluated in the SAR [Safety Analysis 
    Report]. This activity involves changing the allowable operating 
    limit for the Drywell and Suppression Chamber Purge System from 90 
    hours each 365 days to 180 hours each 365 days. This change 
    increases the probability that this system will be in service should 
    a LOCA [loss of coolant accident] occur, but does not increase the 
    probability that a LOCA will occur.
        Increasing the operating limit for the Drywell and Suppression 
    Chamber Purge System from 90 hours to 180 hours each 365 days does 
    not increase the consequences of a LOCA as previously evaluated in 
    the SAR. These proposed TS changes increase the probability of a 
    LOCA occurring during the time the Drywell and Suppression Chamber 
    Purge System is in operation, and therefore, increase the 
    probability of the failure of the operating SGTS [Standby Gas 
    Treatment System] filter bank. However, the risk to containment 
    integrity was previously evaluated and found to be acceptable (UFSAR 
    [Updated Final Safety Analysis Report] Section 9.4.5.1.2.2 and 
    WASH--1400 ``Reactor Safety Study'').
        Increasing the duration that the vent/purge line isolation 
    valves may be open does not increase the probability that these 
    valves will not perform as designed (i.e., close upon receipt of an 
    isolation signal) in response to a LOCA. However, the changes will 
    increase the likelihood that the vent and purge valves will be 
    called on to close. As discussed in UFSAR Section 6.2.4.2, the 
    containment purge valves have undergone extensive testing and 
    analyses to demonstrate the operability of these valves following a 
    LOCA.
        In addition to the existing Safety Analysis Report (SAR) 
    evaluations, a Level 2 PSA [Probabilistic Safety Assessment] 
    Analysis (containment failure) was performed to determine the 
    additional risk associated with changing the operating limit from 90 
    to 180 hours each 365 days. The PSA evaluation conservatively 
    assumed a 200 hour vent/purge duration per a 365 day period. The 
    figure of merit evaluated is the large early release frequency 
    (LERF) which represents the likelihood of containment failure 
    following core damage that could significantly affect the public 
    (e.g., release of a large amount of radioactive material early 
    enough in the accident that evacuation of the public has not 
    occurred). The 200 hour vent/purge duration increased the LERF 
    approximately 3% from the base value of 2.57E-8 for all PSA 
    initiators. This analysis concluded that the increase in risk of 
    containment failure is well within the bounds of the EPRI 
    [Electrical Power Research Institute] PSA Applications Guideline for 
    permanent changes. The same relative increase applies to the large 
    Design Basis Accident LOCA LERF.
        These changes do not directly or indirectly degrade the 
    performance of any other safety systems (assumed to function in the 
    accident analysis) below their design basis. The potential for other 
    equipment failures in the reactor enclosure due to duct-work impact, 
    impingement, and the resulting environmental conditions was 
    evaluated. It was concluded that the environmental qualifications 
    for the LGS equipment are sufficient to ensure operability under the 
    predicted environmental conditions, and there is no impact or 
    impingement-related damage to essential equipment. Although the 
    probability of occurrence of a malfunction of equipment important to 
    safety is increased, the existing SAR analysis and Level 2 PSA 
    Analysis demonstrate the increased risk and radiological 
    consequences are not significant.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        This activity does not change the function of the Drywell and 
    Suppression Chamber Purge System, the containment isolation system, 
    or SGTS as previously evaluated in the SAR. Changing the duration of 
    operation of the vent and purge system does not create an accident 
    initiator not considered in the SAR. Therefore, the possibility of 
    an accident of a different type is not created.
        This activity does not create a failure mode not considered in 
    the SAR. All possible equipment failures that could occur as a 
    result of a LOCA during high volume purging have previously been 
    identified and evaluated in the SAR. Therefore, this activity does 
    not create the possibility of a different type of malfunction of 
    equipment important to safety.
        Therefore, the proposed TS changes will not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The Bases of Technical Specification 3.6.1.8 states that the 
    intent of the 90 hour per 365 day operating limit for the Drywell 
    and Suppression Chamber Purge System is to protect the integrity of 
    the SGTS filters. As discussed above, the requirements specified in 
    ODCM paragraph 3.3.6 assure the availability of the backup SGTS 
    filter train during operation of the vent and purge system. 
    Furthermore, as discussed above, revising the operating limit from 
    90 hours to 180 hours each 365 days does not involve a significant 
    increase in risk. The margin of safety as defined in the Bases of 
    Technical Specification 3.6.1.8 is maintained.
        Therefore, the implementation of the proposed TS changes will 
    not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: John F. Stolz.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment request: February 6, 1996.
        Description of amendment request: The amendments would change the 
    Technical Specifications to lower the 125 Volt Battery Charger 
    surveillance amperage from at least 200 amps to at least 170 amps.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed amendment will permit replacement of aging battery 
    chargers while ensuring these replacement battery chargers will 
    restore the battery from the design minimum charge to its fully 
    charged state while supplying normal steady-state loads. This meets 
    the design basis for the 125V DC system and is consistent with Salem 
    Unit 1 and 2 commitment to IEEE 308-1971 in UFSAR Section 3A.
        The 125V DC battery chargers are not addressed as a contributor 
    to any accident analyzed in the UFSAR, therefore, changes to the 
    battery charger output current will not increase the probability of 
    an accident occurring.
        The limiting analyzed accident considered in this proposed TS 
    amendment is the Loss of Offsite Power coincident with a Loss of 
    Coolant Accident. This is currently the limiting design duty cycle 
    for the batteries. The 125V batteries are sized to maintain all 
    emergency loads for a period of 2 hours without battery chargers. 
    This is demonstrated by performing the surveillance specified in TS 
    4.8.2.3.2.f, which is not being changed. Since the chargers are not 
    required to be available during this 2 hour period, and since the 
    proposed charging rate will supply the necessary loads following 
    restoration of AC power, the proposed amendment will have no effect 
    on the consequences of this accident.
        The current limiter is calculated to extend the recharging time 
    from 20 hours to 30 hours, but this is not considered significant 
    since two, sequential battery discharge events are not considered 
    plausible.
        PSE&G calculation substantiates the capability of the chargers 
    to restore the battery from the design minimum charge to its fully 
    charged state while supplying 
    
    [[Page 7557]]
    normal steady-state loads following a Station Blackout (SBO) Event 
    which exceeds the current design duty cycle.
        In addition, a review of 125V DC Battery System load profiles 
    indicated that the battery chargers are capable of supplying 
    expected loads when restoring the battery from a design minimum 
    charge state to a fully charged state irrespective of the status of 
    the plant.
        Therefore, the proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed amendment does not result in any design or physical 
    configuration changes to the 125V DC system. This change supports 
    the installation of the replacement chargers and ensures the 
    chargers are surveilled within the bounds of limiting input 
    amperage. No changes are being made to the function, design basis, 
    or operation of the 125V DC system by this proposed change. 
    Therefore, the proposed amendment will not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. Will not involve a significant reduction in a margin of 
    safety.
        The proposed amendment to TS 4.8.2.3.2.e ensures that the 
    replacement battery chargers have sufficient capacity to restore 
    each 125V battery from the design minimum charge to its fully 
    charged state while supplying normal steady-state loads. A margin of 
    safety is maintained on both the AC input and DC output of the 
    chargers since the specified current is above that required to 
    support the 125V DC system and will result in AC current below the 
    ampacity rating of the battery charger input cables.
        Testing to a charger output current of at least 170 amps will 
    maintain a margin of safety to the current required during actual 
    worst case normal loading on the 125V DC buses.
        Therefore, the proposed amendment will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502.
        NRC Project Director: John F. Stolz.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. Ginna 
    Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: February 9, 1996.
        Description of amendment request: The proposed amendment would 
    allow an installed overhead door assembly, to be used in lieu of the 
    equipment hatch closure, to isolate the hatch opening to the 
    containment building during fuel movement and core alterations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated. Containment 
    closure is used with respect to the mitigation of fuel handling 
    accidents, and as such, any change to these requirements will not 
    affect the probability of an accident. The proposed changes will 
    also not result in a significant increase in the consequences of an 
    accident previously analyzed since the technical specification 
    requirements remain bounded by the fuel handling accident assumption 
    of no containment closure.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The proposed 
    changes do not involve a physical alteration of the plant (i.e., no 
    new or different type of equipment will be installed) or changes in 
    the methods governing normal plant operation. The proposed changes 
    will not impose any new or different requirements. Thus, this change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety. Containment closure is not assumed in the accident analyses 
    for Ginna Station. Also, the proposed change remains acceptable with 
    respect to SRP [NUREG-800, ``Standard Review Plan for the Review of 
    Safety Analysis Reports for Nuclear Power Plants, July 1981''] 
    15.7.4 and GDC [General Design Criterion] 19 requirements. 
    Therefore, no question of safety is involved, and the change does 
    not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005.
        NRC Project Director: Ledyard B. Marsh.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R.E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: February 9, 1996.
        Description of amendment request: The proposed amendment would 
    incorporate the methodology for determining the Low Temperature 
    Overpressure Protection (LTOP) limits into the Administrative Controls 
    Section 5.6.6 of the Ginna Technical Specifications (TS). The proposed 
    amendment will allow the licensee to perform future LTOP evaluations, 
    using NRC-approved methodology, without requiring changes to the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated. The proposed 
    changes only require that future LTOP limits be developed using NRC 
    approved methodology as specified within the Administrative Controls 
    section and do not involve any technical changes. As such, these 
    changes are administrative in nature and do not impact initiators or 
    analyzed events or assumed mitigation of accident or transient 
    events. Therefore, these changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The proposed 
    changes do not involve a physical alteration of the plant (i.e., no 
    new or different type of equipment will be installed) or changes in 
    the methods governing normal plant operation. The proposed changes 
    will not impose any new or different requirements. Thus, this change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety. The proposed changes will not reduce a margin of plant 
    safety because 
    
    [[Page 7558]]
    the changes do not impact any safety analysis assumptions other than 
    requiring future evaluations of LTOP limits to be performed in 
    accordance with NRC approved methodology. These changes are 
    administrative in nature. As such, no question of safety is 
    involved, and the change does not involve a significant reduction in 
    a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005.
        NRC Project Director: Ledyard B. Marsh.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R.E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: February 9, 1996.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications setpoints for steam generator (SG) 
    water level-high feedwater isolation function. It would take advantage 
    of a greater allowable operating band for SG water level afforded by 
    replacement SGs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated. The proposed 
    setpoint change does not degrade the performance of any plant 
    equipment. Therefore, the probability of an accident is not 
    increased. Since the revised trip setpoint and allowable value 
    remain bounded by the accident analysis value of 100% steam 
    generator narrow range level, the consequences of any accident are 
    not adversely affected.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The proposed 
    change does not involve a physical alteration to the plant (i.e., no 
    new or different types of equipment will be installed) or changes in 
    the methods governing normal plant operation. Thus, this change does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety. The revised setpoint and allowable value remain bounded by 
    the accident analysis assumptions. The existing values are based on 
    design considerations and not accident analysis parameters. The 
    replacement steam generators are not restricted by the same design 
    considerations with respect to the ESFAS [engineered safety features 
    actuation system] Steam Generator Water Level--High function. 
    Therefore, this change does not involve a reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005.
        NRC Project Director: Ledyard B. Marsh.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: February 9, 1996.
        Description of amendment request: The proposed amendment would 
    change Technical Specification 5.3.1 to allow the use of Zirlo fuel 
    cladding material.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The methodologies used in the accident analysis remain 
    unchanged. The proposed changes do not change or alter the design 
    assumptions for the systems or components used to mitigate the 
    consequences of an accident. Use of ZIRLO fuel cladding does not 
    adversely affect fuel performance or impact nuclear design 
    methodology. Therefore accident analyses are not impacted.
        The operating limits will not be changed and the analysis 
    methods to demonstrate operation within the limits will remain in 
    accordance with NRC approved methodologies. Other than the changes 
    to the fuel assemblies, there are no physical changes to the plant 
    associated with this technical specification change. A safety 
    analysis will continue to be performed for each cycle to demonstrate 
    compliance with all fuel safety design bases.
        VANTAGE 5 fuel assemblies with ZIRLO clad fuel rods meet the 
    same fuel assembly and fuel rod design bases as other VANTAGE 5 fuel 
    assemblies. In addition, the 10 CFR 50.46 criteria are applied to 
    the ZIRLO clad rods. The use of these fuel assemblies will not 
    result in a change to the reload design and safety analysis limits. 
    Since the original design criteria are met, the ZIRLO clad fuel rods 
    will not be an initiator for any new accident. The clad material is 
    similar in chemical composition and has similar physical and 
    mechanical properties as Zircaloy-4. Thus, the cladding integrity is 
    maintained and the structural integrity of the fuel assembly is not 
    affected. ZIRLO cladding improves corrosion performance and 
    dimensional stability. No concerns have been identified with respect 
    to the use of an assembly containing a combination of Zircaloy-4 and 
    ZIRLO clad fuel rods. Since the dose predictions in the safety 
    analyses are not sensitive to fuel rod cladding material, the 
    radiological consequences of accidents previously evaluated in the 
    safety analysis remain valid.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        VANTAGE 5 fuel assemblies with ZIRLO clad fuel rods satisfy the 
    same design bases as those used for other VANTAGE 5 fuel assemblies. 
    All design and performance criteria continue to be met and no new 
    failure mechanisms have been identified. The ZIRLO cladding material 
    offers improved corrosion resistance and structural integrity.
        The proposed changes do not affect the design or operation of 
    any system or component in the plant. The safety functions of the 
    related structures, systems or components are not changed in any 
    manner, nor is the reliability of any structure, system or component 
    reduced. The changes do not affect the manner by which the facility 
    is operated and do not change any facility design feature, structure 
    or system. No new or different type of equipment will be installed. 
    Since there is no change to the facility or operating procedures, 
    and the safety functions and reliability of structures, systems or 
    components are not affected, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Use of ZIRLO cladding material does not change the VANTAGE 5 
    reload design and safety limits. The use of these fuel assemblies 
    will take into consideration the normal core operating conditions 
    allowed in the Technical Specifications. For each cycle reload core, 
    the fuel assemblies will be 
    
    [[Page 7559]]
    evaluated using NRC-approved reload design methods, including 
    consideration of the core physics analysis peaking factors and core 
    average linear heat rate effects.
        The use of Zircaloy-4, ZIRLO or stainless steel filler rods in 
    fuel assemblies will not involve a significant reduction in the 
    margin of safety because analyses using NRC-approved methodologies 
    will be performed for each configuration to demonstrate continued 
    operation within the limits that assure acceptable plant response to 
    accidents and transients. These analyses will be performed using 
    NRC-approved methods that have been approved for application to the 
    fuel configuration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street NW., Washington, D.C. 20037.
        NRC Project Director: William H. Bateman.
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: January 30, 1996.
        Description of amendment request: The proposed amendments would 
    modify the Technical Specifications to increase the minimum allowable 
    reactor coolant system total flow rate from 284,000 gpm (for Unit 1) 
    and 275,300 gpm (for Unit 2) to 295,000 gpm for both units. Through the 
    1980's and into the 1990's the North Anna Unit 1 and 2 steam generators 
    experienced increasing levels of steam generator tube plugging. There 
    was a corresponding decrease in the reactor coolant flow rate. As a 
    result, the Commission issued several amendments in the 1989 to 1992 
    time frame to reduce the minimum reactor coolant flow rate. 
    Subsequently, the licensee replaced the steam generators in both units, 
    with steam generators having an increased number of tubes compared to 
    the replaced steam generators. With the increased number of tubes and 
    less flow resistance, a greater reactor coolant flow rate is 
    attainable. When the amendments were issued decreasing the minimum 
    required reactor coolant flow rate, the transmittal letters stated the 
    revision was temporary and would be increased when the steam generators 
    were replaced.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The probability of occurrence or the consequences of an 
    accident or malfunction of equipment important to safety previously 
    evaluated in the safety analysis report would not increase. The 
    proposed Technical Specifications change only increases the minimum 
    allowable RCS total flow rate in the applicable Limiting Condition 
    of Operation. No other changes are being made to allowable operating 
    conditions defined by Technical Specifications, procedures, or to 
    any plant design feature by the implementation of this change. There 
    is no impact on the actual plant performance. Changes in the assumed 
    initial conditions for the accident have no bearing on the 
    probability of occurrence of the assumed accident or malfunction. 
    The RCS flow rate is an assumption in applicable safety analyses. 
    Existing analyses of record have assumed RCS flow rates which are 
    bounding with respect to expected actual plant behavior. Therefore, 
    the implementation of the proposed Technical Specifications change 
    does not affect the probability nor increase the consequences of an 
    accident previously evaluated.
        2. The possibility for an accident or malfunction of a different 
    type than any evaluated previously in the safety analysis report 
    would not be created. The proposed change to North Anna Units 1 and 
    2 Technical Specifications Table 3.2-1 does not involve any 
    alterations to the physical plant which would introduce any new or 
    unique operational modes or accident precursors. Only the allowable 
    value for measured Reactor Coolant System Total Flow Rate will be 
    changed.
        3. The margin of safety as defined in the basis for any 
    technical specifications is not reduced. The proposed Technical 
    Specifications change only increases the minimum allowable RCS total 
    flow rate in the applicable Limiting Condition of Operation. The RCS 
    flow rate is an assumption in applicable safety analyses. Existing 
    analyses of record have assumed RCS flow rates which are bounding 
    with respect to expected actual plant behavior. Therefore, the 
    margin of safety is not reduced by the proposed increase in the 
    allowable RCS Total Flow Rate.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews.
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: January 31, 1996.
        Description of amendment request: The amendments would revise the 
    Technical Specifications to reduce the minimum volume of fuel that must 
    be maintained in the diesel generator day tanks from 750 to 450 
    gallons. The amendments would also revise the surveillance requirements 
    for the diesel generators to permit some surveillances to be performed 
    while the reactor units are at power where the licensee considers it 
    safe to do so without compromising the availability of the diesel 
    generators to perform their intended function.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve an increase in the probability of occurrence of an 
    accident previously evaluated.
        The proposed changes do not result in any physical modifications 
    to any plant systems or components nor change the operation of any 
    plant equipment. The EDG [emergency diesel generator] fuel oil 
    supply system will continue to provide adequate fuel supply to the 
    EDGs in a manner consistent with applicable accident analyses. 
    Performing surveillance tests or portions of surveillance tests at 
    power that do not jeopardize stable plant operations does not 
    increase the probability of occurrence of previously analyzed 
    accidents.
        Therefore, there is no increase in the probability of occurrence 
    of any accident.
        2. Increase the consequences of an accident previously 
    evaluated.
        The proposed changes do not result in any physical modifications 
    to any plant systems or components nor change the operation of any 
    plant equipment. The EDG fuel oil system remains capable of 
    supplying the EDGs with sufficient quantities of fuel oil to provide 
    power for long term loss of offsite power. The EDG surveillances 
    will continue to be performed in a manner that will ensure that the 
    EDGs will be capable of performing their intended safety functions. 
    The proposed changes to the electrical distribution system 
    surveillances will continue to ensure that the electrical 
    distribution system remains 
    
    [[Page 7560]]
    operable to power the required safety systems.
        Therefore, these proposed changes will not result in an increase 
    in the consequences of any evaluated accidents.
        3. Create the possibility for an accident of a different type 
    than was previously evaluated.
        The proposed changes do not result in any physical modifications 
    to any plant systems or components nor change the operation of any 
    plant equipment. Only those surveillance tests or portions of 
    surveillance tests that do not jeopardize stable plant operation 
    will be performed at power. Overlap testing to fully test the 
    electrical distribution system protection functions does not 
    introduce any unique accident precursors. The EDG fuel oil system 
    remains capable of supplying the EDGs with sufficient quantities of 
    fuel oil to provide power for long term loss of offsite power. The 
    EDG surveillances will continue to be performed in a manner that 
    will ensure that the EDGs will be capable of performing their 
    intended safety functions.
        Therefore, there are no new precursors generated that would 
    result in the possibility of a different type of an accident than 
    was previously evaluated in the SAR [Safety Analysis Report].
        4. Decrease the margin of safety as described in the bases 
    section of Technical Specifications.
        The EDG fuel oil system will continue to provide adequate fuel 
    supply in a manner consistent with applicable accident analyses. The 
    EDG surveillances will continue to be performed in a manner that 
    will ensure that the EDGs are capable of performing their intended 
    safety functions. The proposed changes to the electrical 
    distribution system surveillances will continue to ensure that the 
    electrical distribution system remains operable to power the 
    required safety systems.
        Therefore, the margin of safety as described in the Technical 
    Specifications is not reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of application for amendment: July 21, 1995, August 8, 1995, 
    and December 15, 1995.
        Brief description of amendment request: The proposed amendment 
    would modify the requirements for testing an emergency diesel generator 
    (EDG) when the other is inoperable. The amendment would correct an 
    editorial error in the Duane Arnold Energy Center Operating License and 
    would correct an erroneous reference in the Technical Specification.
        Date of publication of individual notice in Federal Register: 
    February 2, 1996 (61 FR 3953).
        Expiration date of individual notice: March 4, 1996.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401.
    
    Pacific Gas and Electric Company, Docket No. 50-275, Diablo Canyon 
    Nuclear Power Plant, Unit No. 1, San Luis Obispo County, California
    
        Date of amendment request: January 18, 1995.
        Description of amendment request: The proposed amendment would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Nuclear Power Plant, Unit Nos. 1 and 2, to allow operation of Unit 1 in 
    Mode 3 (Hot Standby) during replacement of nonvital auxiliary 
    transformer 1-1. Specifically, TS 3/4.8.1.1, ``Electrical Power 
    Systems--A.C. Sources--Operating,'' Action Statement (a), would be 
    revised to permit a one-time extension of the allowed outage time (AOT) 
    from 72 hours to 120 hours.
        Date of individual notice in Federal Register: February 1, 1996 (61 
    FR 3737).
        Expiration of individual notice: March 4, 1996.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: February 5, 1996, as supplemented by 
    letter dated February 14, 1996.
        Brief description of amendment request: The amendment changes 
    Technical Specifications 4.6.2.3.b, ``Suppression Pool Cooling'', and 
    TS 4.6.2.2.b, ``Suppression Pool Spray'', to include flow through the 
    RHR heat exchanger bypass line (in addition to the RHR heat exchanger) 
    in the Suppression Pool Cooling and Suppression Pool Spray flow path 
    used during RHR pump testing.
        Date of publication of individual notice in Federal Register: 
    February 9, 1996 (61 FR 5040).
        Expiration date of individual notice: March 11, 1996.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: January 16, 1996.
        Brief description of amendment request: The proposed amendment 
    would change the Technical Specification surveillance frequency for the 
    drywell bypass leakage rate test from 18 months to 120 months (10 
    years) with a more frequent testing requirement if performance 
    degrades. Additionally, specific leakage limits would be deleted for 
    the air lock seal and barrel tests. Also, surveillance frequencies for 
    the air lock interlock test and seal pneumatic system leak test would 
    be changed from 18 months to 24 months. Finally, the surveillance 
    frequencies for the air lock barrel test would be changed from ``each 
    COLD SHUTDOWN if not performed within 
    
    [[Page 7561]]
    the previous 6 months'' to ``at least once per 24 months'' and from 18 
    months to 24 months. The licensee requested that this amendment be 
    approved for use during the current refueling outage which began on 
    January 27, 1996.
        Date of publication of individual notice in Federal Register: 
    February 2, 1996 (61 FR 3951).
        Expiration date of individual notice: March 4, 1996.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit No. 1, Calvert County, 
    Maryland
    
        Date of application for amendments: December 7, 1995.
        Brief description of amendments: The amendments add the convolution 
    analytical technique for the analysis of the pre-trip main steam line 
    break event to the list of approved core operating limits analytical 
    methods listed in Technical Specification 6.9.1.9, ``Core Operating 
    Limits Report.'' The convolution analytical technique was previously 
    reviewed and approved by the NRC staff and the supporting safety 
    evaluation was provided to Baltimore Gas and Electric Company by letter 
    dated May 11, 1995.
        Date of issuance: February 5, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 210 and 188.
        Facility Operating License No. DPR-53 and DPR-69: Amendment revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    177)
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated February 5, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: November 2, 1994, as 
    supplemented by letters dated November 16 and December 14, 1995.
        Brief description of amendments: The amendments delete the content 
    of the Appendix B, ``Environmental Protection Plan'' (Non-radiological) 
    Technical Specifications and modify License Condition 2.C.(2) so as to 
    delete that portion which refers to the Environmental Protection Plan.
        Date of issuance: February 5, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1-164--Unit 2-146.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications and License Conditions.
        Date of initial notice in Federal Register: March 1, 1995 (60 FR 
    11131). The November 16 and December 14, 1995, letters provided 
    clarifying information that did not change the scope of the November 2, 
    1994, application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 5, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: January 13, 1995, as 
    supplemented by letter dated August 30, 1995.
        Brief description of amendments: The amendments revise the 
    Technical Specifications to increase the surveillance test intervals 
    and allowed outage times for the Reactor Trip System and Engineered 
    Safety Features Actuation System. The NRC staff has reviewed the 
    proposed changes and finds that, with one exception as noted in the 
    enclosed Safety Evaluation, the amendments conform to WCAP-10271, 
    ``Evaluation of Surveillance Frequencies and Out of Service Times for 
    the Reactor Protection Instrumentation Systems,'' with its revisions 
    and supplements, provides appropriate limiting conditions for operation 
    and action statements, and is, therefore acceptable.
        Date of issuance: February 16, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1-165--Unit 2-147.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 15, 1995 (60 FR 
    14019).
        The August 30, 1995, letter provided clarifying information that 
    did not change the scope of the January 13, 1995, application and the 
    initial proposed no significant hazards consideration determination. 
    The Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated February 16, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
    
    [[Page 7562]]
    
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: July 10, 1995.
        Brief description of amendments: These amendments modify the 
    Technical Specifications to minimize the potential for boron dilution 
    of the reactor coolant system (RCS) during startup of an isolated RCS 
    loop. The changes permit RCS loop isolation only during Modes 5 and 6 
    and require the RCS loop isolation valves be open with power removed 
    from their valve operators during Modes 1, 2, 3, and 4. The changes 
    also require isolation of primary grade water from the RCS during Modes 
    4, 5, and 6, except during planned boron dilution or makeup activities.
        Date of issuance: February 12, 1996.
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment Nos.: 195 and 78.
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42602).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 12, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of application for amendments: July 20, 1995, as supplemented 
    December 4, 1995.
        Brief description of amendments: These amendments revise Technical 
    Specification 3/4.8.1.1, ``A.C. Sources-Operating,'' to incorporate 
    guidance provided in NRC Generic Letter (GL) 84-15, ``Proposed Staff 
    Actions to Improve and Maintain Diesel Generator Reliability,'' and GL 
    93-05, ``Line-Item Technical Specification Improvements to Reduce 
    Surveillance Requirements for Testing During Power Operation,'' which 
    includes (1) revised requirements for testing the operable emergency 
    diesel generators (EDGs) for various combinations of inoperable offsite 
    circuits and EDGs and (2) revised surveillance requirements for the 
    EDGs. The revised surveillance requirements include specifying 
    generator voltage, frequency limits, and diesel starting time. The 
    amendments also make several editorial changes to TS 3/4.8.1.1 to make 
    TS 3/4 8.1.1 consistent with the guidance provided in the NRC's 
    Improved Standard Technical Specifications (NUREG-1431).
        Date of issuance: February 12, 1996.
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment Nos.: 196 and 79.
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42603).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 12, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: B.F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: November 22, 1995.
        Brief description of amendments: The amendments consist of changes 
    relating to removal of the TS Bases from the TS index.
        Date of issuance: February 13, 1996.
        Effective date: February 13, 1996.
        Amendment Nos.: 182 and 176.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65678).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 13, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Unit No. 3 Nuclear Generating Plant, Citrus County, Florida
    
        Date of application for amendment: May 31, 1995, as supplemented 
    November 28, 1995, and December 21, 1995. The supplementary submittals 
    did not affect the staff's proposed finding of no significant hazards 
    consideration.
        Brief description of amendment: This amendment increases the 
    surveillance interval on various instruments from 18 to 24 months.
        Date of issuance: February 13, 1996.
        Effective date: February 13, 1996.
        Amendment No.: 152.
        Facility Operating License No. DPR-72. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35070).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 13, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: October 16, 1995, as 
    supplemented by letter dated December 22, 1995.
        Brief description of amendments: The amendments add a footnote to 
    Technical Specification 4.6.1.2.d stating the Type B and C tests 
    scheduled for Unit 1's refueling outage, cycle 6 (1R6) will be 
    conducted in accordance with Option B of 10 CFR Part 50, Appendix J 
    (hereafter referred to as Option B) using the guidance of Regulatory 
    Guide 1.163, September 1995. This change only applies to Unit 1's 
    refueling outage 1R6 because implementation of Option B for Type A, B, 
    and C testing for both units is being incorporated into the Improved TS 
    that are scheduled to become effective after refueling outage 1R6.
        Date of issuance: February 2, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1-93--Unit 2-71.
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62490).
        The December 22, 1995, letter provided clarifying information that 
    did not change the scope of the October 16, 1995, application and the 
    initial proposed no significant hazards consideration determination. 
    The Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated February 2, 1996. 
    
    [[Page 7563]]
    
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: June 9, 1995, as supplemented 
    November 9, 1995.
        Brief description of amendment: The amendment relocates 
    Surveillance Requirement 4.6.6.1.d.3 to TS 3.6.6.2 and revises the 
    Action Statement of Section 3.6.6.1 to decouple it from Section 
    3.6.6.2. In addition, Definition 1.12, ``Secondary Containment 
    Boundary'' is deleted and included in the Bases Section 3/4.6.6, 
    Secondary Containment. Bases Section 3/4.6.6.2, Secondary Containment 
    is expanded using the guidance of the improved standard technical 
    specifications (STS) for Westinghouse plants (NUREG-1431).
        Date of issuance: February 5, 1996.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 126.
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39445).
        The November 9, 1995, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 5, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community--Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota.
    
        Date of application for amendments: July 17, 1995, as supplemented 
    October 16, 1995, and November 28, 1995.
        Brief description of amendments: The amendments revise the Prairie 
    Island Radiological Effluent Technical Specifications and other 
    sections relating to radiological controls to conform to NUREG-1431, 
    ``Standard Technical Specifications, Westinghouse Plants,'' Revision 1, 
    and Generic Letter 89-01, ``Implementation of Programmatic Controls for 
    Radiological Effluent Technical Specifications in the Administrative 
    Controls Section of the Technical Specifications and the Relocation of 
    Procedural Details of RETS to the Offsite Dose Calculation Manual or to 
    the Process Control Program.''
        Date of issuance: January 24, 1996.
        Effective date: January 24, 1996, with full implementation within 
    120 days.
        Amendment Nos.: Unit 1-122; Unit 2-115.
        Facility Operating License Nos. DPR-42 and DPR-60. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52933).
        By letters of October 16, 1995, and November 28, 1995, NSP 
    forwarded a copy of its revised ODCM to the NRC for use as a reference 
    and provided additional clarifying information. This information did 
    not change the licensee's amendment request, the scope of the original 
    Federal Register notice or the staff's initial proposed no significant 
    hazards considerations determination. Therefore, renoticing was not 
    warranted. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 24, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: July 28, 1995.
        Brief description of amendments: The amendment eliminates the 
    Technical Specifications requirements to perform 10 CFR Part 50, 
    Appendix J, Type C hydrostatic tests on certain valves that are assured 
    a water seal following a Design Basis Accident.
        Date of issuance: February 8, 1996.
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment Nos.: 110 and 73.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49941).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 8, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick 
    Generating Station, Unit 1, Montgomery County, Pennsylvania.
    
        Date of application for amendment: June 19, 1995, as supplemented 
    December 21, 1995.
        Brief description of amendment: The amendment revises Technical 
    Specification Section 2.2, ``Safety Limits,'' to change the minimum 
    critical Power ratio safety Limit due to use of General Electric 13 
    fuel product line.
        Date of issuance: February 8, 1996.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days.
        Amendment No. 111.
        Facility Operating License No. NPF-39. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52934).
        The December 21, 1995, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination nor the Federal Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 8, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: July 28, 1995.
        Brief description of amendments: The amendments delete the 
    operability and surveillance requirements involving secondary 
    containment differential pressure instrumentation.
        Date of issuance: As of date of issuance, to be implmented within 
    30 days.
        Effective date: February 14, 1996.
        Amendment Nos.: 112 and 74.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications. 
    
    [[Page 7564]]
    
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49942).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 14, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: July 28, 1995.
        Brief description of amendments: These amendmends revise Technical 
    Specifications Table 4.3.1.1-1, ``Reactor Protection System 
    Instrumentation Surveillance Requirements,'' to reflect changes the 
    surveillance test frequency requirements for various Reactor Protection 
    System instrumentation.
        Date of issuance: February 14, 1996.
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment Nos.: 113 and 75.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49944).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 14, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: January 20, 1995, as 
    supplemented by letter dated December 18, 1995.
        Brief Description of amendment: The Technical Specification (TS) 
    revision represents changes to TS Section 3/4.11.2.6, ``Explosive Gas 
    Mixture,'' TS Table 3.3.7.11-1, ``Radioactive Gaseous Effluent 
    Monitoring Instrumentation,'' and TS Table 4.3.7.11-1, ``Radioactive 
    Gaseous Effluent Monitoring Instrumentation Surveillance 
    Requirements.'' The revision removes these TS from the Technical 
    Specifications and relocates the Bases to the Hope Creek Updated Final 
    Safety Analysis Report and the Surveillance Requirements to the 
    applicable surveillance procedures. The Limiting Conditions for 
    Operation are eliminated.
        Date of issuance: February 6, 1996.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 91.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39452)
        The December 18, 1995 supplement did not effect the proposed no 
    significant hazards determination, contained in the January 20, 1995 
    application or the Federal Register notice (60 FR 39452).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 6, 1996
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: October 7, 1995 as supplemented 
    by letter dated October 27, 1995.
        Brief description of amendment: This amendment changes Technical 
    Specification (TS) 4.8.1.1.2, ``A.C. Sources--Operating,'' by replacing 
    the reference to an upper voltage and frequency band for the 10-second, 
    Emergency Diesel Generator (EDG), starting time test with a minimum 
    required voltage and frequency that must be attained within 10 seconds. 
    The change to TS 4.8.1.1.2 also includes several related changes to TS 
    4.8.1.1.2 as follows: (1) the requirement for an EDG to achieve 514 
    rpm, within 10 seconds following a start signal during testing is 
    eliminated, (2) the term ``standby'' replaces the term ``ambient'' in 
    describing the EDG test restart condition, and (3) the term ``must'' is 
    replaced with the term ``may'' in describing the use of manufacturers 
    recommendations for EDG loading.
        Date of issuance: February 6, 1996.
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment No.: 92.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 27, 1995 (60 
    FR 58405)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 6, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: May 26, 1995, as supplemented 
    May 5, 1995, and January 26, 1996.
        Brief description of amendment: The proposed change was to allow 
    the storage of fuel with an enrichment not to exceed a nominal 5.0 
    weight percent (w/o) Uranium-235 (U-235) in the new (fresh) and spent 
    fuel storage racks and change the license to reflect changes related to 
    the nuclear fuel cycle.
        Date of issuance: February 6, 1996.
        Effective date: February 6, 1996.
        Amendment No.: 60.
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications and License.
        Date of initial notice in Federal Register: September 26, 1995 (60 
    FR 49636)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 6, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: May 26, 1995, as supplemented by 
    letters dated July 17, August 14, August 31, September 18, October 6, 
    October 18, November 1, November 16, two letters of November 20, 
    November 21, November 22, two letters of November 27, November 30, 
    December 8, and December 28, 1995; and November 27, 1995; and May 23, 
    1994, as supplemented by letters dated June 15, 1994, July 11, July 15, 
    November 1, and November 16, 1995; and September 15, 1992, as 
    supplemented April 20, 1993, April 26, 1995, and July 27, 1995.
        Brief description of amendment: (1) a full conversion from the 
    licensee's current Technical Specifications (TSs) to a set of TSs based 
    on NUREG-1431, 
    
    [[Page 7565]]
    ``Standard Technical Specifications, Westinghouse Plants,'' Revision 0, 
    dated September 1992 (including approved travellers used in the 
    issuance of Revision 1, dated April 1995), in response to the 
    licensee's application dated May 26, 1995, as supplemented by letters 
    dated July 17, August 14, August 31, September 18, October 6, October 
    18, November 1, November 16, two letters of November 20, November 21, 
    November 22, two letters of November 27, November 30, December 8, and 
    December 28, 1995. (2) a revision to the TSs to implement the amended 
    regulation 10 CFR Part 50, Appendix J, Option B (new rule), to provide 
    a performance based option for leakage-rate testing of containment, in 
    response to the licensee's application dated November 27, 1995. (3) a 
    revision to the TSs regarding allowable primary coolant levels of 
    specific activity, in response to the licensee's application dated May 
    23, 1994, as supplemented by letters dated June 15, 1994, July 11, July 
    15, November 1, and November 16, 1995. (4) a revision to the TSs adding 
    new requirements that enhance the reliability of power-operated relief 
    valves and block valves (PORV/BV) along with TS changes that provide 
    additional low-temperature overpressure protection, in response to the 
    licensee's application dated September 15, 1992, as supplemented April 
    20, 1993, and April 26, 1995. By letter dated July 27, 1995, the 
    licensee withdrew this amendment request; however, the licensee 
    rescinded this withdrawal request by letter dated December 28, 1995. 
    Therefore, the proposed changes to the PORV/BV, as requested in the 
    licensee's letter dated May 26, 1995, as supplemented December 28, 
    1995, are incorporated into this amendment.
        Date of issuance: February 13, 1996.
        Effective date: February 13, 1996.
        Amendment No.: 61.
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications and License.
        Date of initial notice in Federal Register: December 8, 1995 (60 FR 
    63071); September 26, 1995 (60 FR 49636); August 30, 1995 (60 FR 
    45184); July 6, 1994 (59 FR 34669).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 13, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: December 30, 1993, as 
    supplemented by letters dated June 3, 1994, August 25, 1994, January 3, 
    1995, and January 19, 1995.
        Brief description of amendments: The amendments replace, in their 
    entirety, the current technical specifications (TS) with a set of TS 
    based on NUREG-1432, ``Standard Technical Specifications--Combustion 
    Engineering Reactors,'' September 1992.
        Date of issuance: February 9, 1996.
        Effective date: February 9, 1996, to be implemented by August 9, 
    1996.
        Amendment Nos.: Unit 1--Amendment No. 127; Unit 2--Amendment No. 
    116.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49434) The January 3, 1995, and January 19, 1995, supplemental 
    letters provided additional clarifying information and did not change 
    the initial no significant hazards consideration determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated February 9, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: December 8, 1995 (TS 95-24).
        Brief description of amendments: The amendments implement the 
    change to 10 CFR Part 50, Appendix J to incorporate Option B, a 
    voluntary performance-based option, for determining the frequency for 
    performing Type A, B, and C Containment Leak Rate Testing.
        Date of issuance: February 5, 1996.
        Effective date: February 5, 1996.
        Amendment Nos.: 217 and 207.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    182).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 5, 1996.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: December 8, 1995 (TS 95-20).
        Brief description of amendments: The amendments decrease the 
    frequency for conducting air or smoke tests of the containment spray 
    system headers and Residual Heat Removal System headers from every 5 
    years to every 10 years to verify each spray nozzle is unobstructed.
        Date of issuance: February 7, 1996.
        Effective date: February 7, 1996.
        Amendment Nos.: 218 and 208.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    182).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 7, 1996.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: November 22, 1993 supplemented 
    May 5 and December 20, 1995.
        Brief description of amendment: The amendment revised the Technical 
    Specifications to reflect the replacement of analog temperature 
    instrumentation associated with leak detection with digital equipment.
        Date of issuance: January 29, 1996.
        Effective date: January 29, 1996, and implemented not later than 
    120 days following startup from the fifth refueling outage.
        Amendment No.: 79.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 12, 1994 (59 FR 
    24752).
        The Commission's related evaluation of the amendment is contained 
    in a 
    
    [[Page 7566]]
    Safety Evaluation dated January 29, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: November 2, 1995, supplemented 
    January 26, 1996.
        Brief description of amendment: The amendment only revised the 
    containment personnel air lock Technical Specifications and added a 
    license condition to allow the air locks to be open in Modes 4 and 5 
    during core alterations except for movement of recently irradiated 
    fuel. All other provisions of the request are being deferred for 
    further review.
        Date of issuance: February 2, 1996.
        Effective date: To be implemented not later than 90 days after 
    issuance.
        Amendment No. 80.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications and added a license condition.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62497) The supplemental letter provided clarification of administrative 
    controls that will be in place, did not change the initial no 
    significant hazards consideration determination, and was within the 
    scope of the notice issued December 6, 1995.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 2, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: December 30, 1995, as supplemented by 
    letters dated July 28, (TXX-95187), September 14, (TXX-95235), and 
    November 29, 1995 (TXX-95299), and January 2, 1996 (TXX-96-003).
        Brief description of amendments: These changes authorized usage of 
    the high density fuel storage racks, to increase the spent fuel storage 
    capacity, and to adopt the wording, content, and format of the Improved 
    Standard Technical Specifications.
        Date of issuance: February 9, 1996.
        Effective date: February 9, 1996.
        Amendment Nos.: Unit 1--Amendment No. 46; Unit 2--Amendment No. 32.
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6313).
        The additional information contained in the supplemental letters 
    dated July 28, (TXX-95187), September 14, (TXX-95235), and November 29, 
    1995 (TXX-95299), and January 2, 1996 (TXX-96-003), was clarifying in 
    nature and thus, within the scope of the initial notice and did not 
    affect the staff's proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in an Environmental Assessment dated February 9, 1996, and a Safety 
    Evaluation dated February 9, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: September 19, 1995.
        Brief description of amendments: The amendments increase the 
    surveillance test interval for the turbine reheat stop and intercept 
    valves from at least once per 31 days to at least once per 18 months, 
    extend the visual and surface disassembly inspection interval of the 
    turbine reheat stop and intercept valves to 60 months and revise the 
    inspection criteria for the throttle, governor, reheat stop, and reheat 
    intercept valve disassembly inspections.
        Date of issuance: February 8, 1996.
        Effective date: February 8, 1996.
        Amendment Nos.: 195 and 176.
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: October 25, 1995 (60 FR 
    54725).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 8, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: November 20, 1995, as 
    supplemented January 23, 1996.
        Brief description of amendments: The amendments revise the North 
    Anna Units 1 and 2 Technical Specifications to permit the use of 10 CFR 
    Part 50, Appendix J, Option B, Performance-Based Containment Leakage 
    Rate Testing.
        Date of issuance: February 9, 1996.
        Effective date: February 9, 1996.
        Amendment Nos.: 196 and 177.
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65685). The January 23, 1996 supplement provided clarifying 
    information that was within the scope of the December 20, 1995 notice.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 9, 1996.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of no Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date 
    
    [[Page 7567]]
    the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) The 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By March 29, 1996, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the 
    
    [[Page 7568]]
    effectiveness of the amendment. Any hearing held would take place while 
    the amendment is in effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
    
    Duke Power Company, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: February 6, 1996.
        Brief description of amendments: The amendments revised Technical 
    Specification Section 3.16, ``Containment Hydrogen Control Systems.'' 
    The change adds a footnote to TS 3.16.3.b. to allow a one-time outage 
    duration extension in regard to the Containment Hydrogen Control System 
    flow path. This extension is necessary to install and test plant 
    modifications, which will allow the Containment Hydrogen Control System 
    to perform as designed, without the potential for inoperability due to 
    water accumulation in the flow path.
        Date of Issuance: February 7, 1996.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1-214-Unit 2-214-Unit 3-211.
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated 
    February 7, 1996.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691.
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street NW., Washington, DC 20036.
        NRC Project Director: Herbert N. Berkow.
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: February 10, 1996.
        Brief description of amendment: The amendment revises Technical 
    Specifications (TS) Surveillance Requirements 4.7.6.c.2, 4.7.6.d, 
    4.9.11.b.2 and 4.9.11.c regarding the testing methodology utilized by 
    Virgil C. Summer Nuclear Station, which determines the operability of 
    the charcoal filters in the engineering safety features air handling 
    units.
        Date of issuance: February 10, 1996.
        Effective date: February 10, 1996.
        Amendment No.: 131.
        Facility Operating License No. NPF-12: Amendment revises the TS.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration, are contained in a Safety Evaluation dated 
    February 10, 1996.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180.
    
        Dated at Rockville, Maryland, this 21st day of February 1996.
    
        For the Nuclear Regulatory Commission.
    Steven A. Varga,
    Director, Division of Reactor Projects--I/II, Office of Nuclear Reactor 
    Regulation.
    [FR Doc. 96-4342 Filed 2-27-96; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Published:
02/28/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-4342
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
7542-7568 (27 pages)
PDF File:
96-4342.pdf