95-4870. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 60, Number 40 (Wednesday, March 1, 1995)]
    [Notices]
    [Pages 11125-11151]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-4870]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Pubic Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission on NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the 
    [[Page 11126]] Commission to publish notice of any amendments issued, 
    or proposed to be issued, under a new provision of section 189 of the 
    Act. This provision grants the Commission the authority to issue and 
    make immediately effective any amendment to an operating license upon a 
    determination by the Commission that such amendment involves no 
    significant hazards consideration, notwithstanding the pendency before 
    the Commission of a request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from February 3, 1995, through February 16, 1995. 
    The last biweekly notice was published on February 15, 1995 (60 FR 
    8739).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By March 31, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shale be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no [[Page 11127]] significant hazards consideration, the Commission may 
    issue the amendment and make it immediately effective, notwithstanding 
    the request for a hearing. Any hearing held would take place after 
    issuance of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)(v) and 2.714(d).
        For further details with respect to this section, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Unit Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of amendment requests: December 7, 1994.
        Description of amendment requests: The proposed amendment would 
    revise the capacity of the ultimate heat sink (UHS) as described in the 
    bases of Technical Specification 3/4.7.5, ``Ultimate Heat Sink,'' from 
    providing a 27-day cooling water supply to providing a 26-day cooling 
    water supply. In addition, the reference to Regulatory Guide 1.27 in 
    the bases of this TS would also be revised to reference the January 
    1976 revision rather than the March 1974 revision.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis about the issue of no significant hazards 
    consideration, which is presented below:
    
        Standard 1--Does the proposed change involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        The Essential spray pond system and the UHS do not initiate any 
    accidents in Chapters 6 or 15 of the UFSAR [Updated Final Safety 
    Analysis Report]. The justification and basis for the time that the 
    UHS is available is not changed and continues to be consistent with 
    the guidance in Regulatory Guide 1.27. The existing Technical 
    Specification requirements and those components to which they apply 
    are not altered by this Technical Specification amendment. 
    Therefore, the change to the bases for Technical Specification 3/
    4.7.5 does not increase the probability of occurrence or the 
    consequences of any previously evaluated accident.
        Standard 2--Does the proposed change create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated?
        The requirements for Technical Specification 3/4.7.5 are not 
    changed. This amendment has no impact on plant maintenance, testing, 
    shutdown equipment, or component qualification. Therefore, the 
    possibility of a new or different kind of accident is not created by 
    this amendment.
        Standard 3--Does the proposed change involve a significant 
    reduction in a margin of safety?
        The change to the bases for Technical Specification 3/4.7.5 does 
    not significantly alter existing Technical Specification 
    requirements or those coponments to which they apply. The 
    justification and basis for the time that the UHS is available 
    without makeup is not changed and continues to be consistent with 
    the guidance in Regulatory Guide 1.27. Regulatory Guide 1.27 states 
    that ``A capacity less than 30 days may be acceptable if it can be 
    demonstrated that replenishment can be effected to ensure that 
    continuous capability of the sink to perform its safety functions, 
    taking into account the availability of replenishment equipment and 
    limitations that may be imposed on ``freedom of movement'' following 
    an accident.'' This change does not effect the continuous capability 
    of the UHS to perform its safety function of providing decay heat 
    removal capability following an accident. The change updates the 
    design basis of the UHS using more realistic conditions based on 
    plant experience. Therefore, the change in the capacity of the UHS 
    without makeup from 27 days to 26 days will not involve a 
    significant reduction in margin of safety for the ultimate heat 
    sink.
    
        The NRC staff has reviewed the licensees' analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
        Attorney for licensees: Nancy C. Loftin, Esq., Corporation 
    Secretary and Counsel, Arizona Public Service Company, P.O. Box 53999, 
    Mail Station 9068, Phoenix, Arizona 85072-3999.
        NRC Project Director: Theodore R. Quay.
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: June 18, 1992, as supplemented December 
    8, 1992, and revised February 3, 1995.
        Description of amendment request: The proposed Technical 
    Specification (TS) amendment adds limiting conditions of operation and 
    surveillance requirements for the pressurizer power-operated relief 
    valves (PORVs) and their associated block valves whenever average 
    temperature (Tavg) is above 350 degrees F or the reactor is critical. 
    Specifications have also been added for low-temperature overpressure 
    protection whenever Tavg is less than 350 degrees F and the reactor 
    coolant system is not vented to the containment. The February 3, 1995, 
    revision made editorial changes to previous TS pages and made changes 
    to conform with an additional provision of the guidance for 
    surveillance testing of the block valves associated with the 
    pressurizer PORVs. In addition, the licensee has requested an editorial 
    change to TS page 3.1.-11 to revise the references to two figures that 
    have been superseded.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The requested revision does not involve a significant 
    increase in the probability or consequences of an accident 
    previously [[Page 11128]] evaluated. The proposed revision to our 
    previous Technical Specification (TS) change request dated June 18, 
    1992, would help assure the availability of the block valves for 
    accident mitigation. The availability of the block valves for 
    accident mitigation has been found to outweigh any negative safety 
    consequences associated with full cycle testing of a block valve 
    isolating a pressurizer power-operated relief valves (PORV) with 
    ``excessive'' seat leakage. There would be no significant increase 
    in the probability or consequences of an accident previously 
    evaluated since this event is fully bounded by the failing open of a 
    single pressurizer code safety relief valve event which is analyzed 
    in Chapter 15 of the Updated Final Safety Analysis Report. 
    Accordingly, the requested revision will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The requested revision to our previous TS change request does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated. Periodic testing of the 
    block valves in accordance with the requested revision is only 
    intended to assure the functioning and capability of the block 
    valves. The requested revision will only clarify the conditions when 
    block valve surveillance testing is required. The performance of 
    this testing is intended to improve block valve availability and 
    thereby assure the capability of certain accident mitigation 
    strategies identified within Abnormal and Emergency Operating 
    Procedures. Therefore, the requested revision will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The requested revision to our previous TS change request does 
    not involve a significant reduction in the margin of safety. The 
    requested revision is intended to help assure block valve 
    availability to support certain accident mitigation strategies. This 
    additional assurance of block valve availability and functioning 
    increases the margin of safety. Accordingly, the requested revision 
    will not involve a significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
        NRC Project Director: William H. Bateman.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: December 14, 1994.
        Description of amendment request: The proposed amendments would 
    revise technical specifications related to allowed outage times (AOT) 
    and surveillance test intervals (STI) for certain actuation 
    instrumentation in the reactor protection system (RPS), primary 
    containment isolation system (PCIS), emergency core cooling system 
    (ECCS), recirculation pump trip, reactor core isolation cooling (RCIC), 
    control rod withdrawal block, monitoring, and feedwater/main turbine 
    trip systems. These changes are generally consistent with General 
    Electric topical reports which have been reviewed and approved by the 
    NRC. The changes also include revising the Feedwater/Main Turbine Trip 
    LCO 3.3.8 action statement to achieve consistency with existing 
    instrumentation LCOs; deleting the surveillance of the APRM Neutron 
    Flux--High, Setdown functional unit in Operational Condition 1; 
    revising the applicability of the provisions of Specification 4.0.4 to 
    several Reactor Protection System and Control Rod Withdrawal Block 
    Instrumentation surveillance requirements; adding the requirement to 
    perform shiftly channel checks for applicable RPS, PCIS, ECCS, and RCIC 
    instrumentation channels equipped with master trip units; and other 
    changes to correct typographical errors and to delete cycle specific 
    footnotes which are no longer applicable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    It has been determined that the changes do not constitute a 
    Significant Hazards Consideration. Based on the criteria for 
    defining a significant hazards consideration established in 10 CFR 
    50.92, operation of LaSalle County Station Units 1 and 2 in 
    accordance with the proposed amendment will not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        a. The proposed changes increase the STI and AOT for actuation 
    instrumentation supporting RPS, ECCS, Isolation, CRBF, RCIC, ATWS-
    RPT, EOC-RPT, Monitoring, and Feedwater/Main Turbine Trip System 
    Actuation functions. There are no changes in instrumentation 
    configuration and function, and no instrumentation setpoints are 
    changed. Because of this there is no change in the probability of 
    occurrence of an accident or the consequences of an accident or the 
    consequences of malfunction of equipment. With respect to the 
    probability of equipment malfunction, topical reports prepared by GE 
    demonstrate that there is a reduction in scram frequency for the 
    RPS, but in the case of the ECCS there is a small increase in the 
    unavailability of the water injection function. This increase in 
    unavailability was judged acceptable by GE. The NRC concurred with 
    this conclusion in its review and approval of the topical reports. 
    The proposed changes are consistent with the Safety Evaluation 
    Reports issued for the topical reports.
        b. The changes proposed for the Feedwater/Main Turbine Trip LCO 
    action statements provide actions which are consistent with 
    presently existing instrumentation LCOs. The design and function of 
    the feedwater/main turbine trip instrumentation to trip the 
    feedwater pumps and the main turbine upon detection of a Level 8 
    event is not altered. The probability and/or consequences of this 
    moderate frequency transient are not increased.
        c. The APRM Neutron Flux--High, Setdown scram setting provides 
    adequate thermal margin between the setpoint and the safety limits 
    for operation at low pressure and low flow during a plant startup. 
    This function remains in effect until the mode switch is placed in 
    the Run (Operational Condition 1) position, at which time it is 
    bypassed. Deleting the requirement for the surveillance of the APRM 
    Neutron Flux--High, Setdown functional unit in Operational Condition 
    1 is appropriate since its function is not applicable in this mode. 
    This deletion serves to achieve consistency between Technical 
    Specification Tables and the Bases section.
        d. The changes associated with Specification 4.0.4 are 
    administrative in nature and are intended to provide the plant 
    operators with better guidance for its application. In cases where 
    complete surveillances cannot be achieved, such as during a plant 
    shutdown, then the required surveillances will be performed within 
    24 hours of entering the Mode or condition in which the surveillance 
    is required. The stabilization of the plant will be of primary 
    consideration. This change does not affect the evaluation for any 
    accident presented in Chapter 15 of the UFSAR. The APRM Fixed 
    Neutron Flux--High quarterly functional tests most of the APRM 
    channel equipment associated with the APRM Neutron Flux--High, 
    Setdown scram.
        Additionally, the expected result of the functional tests 
    associated with the SRMs, IRMs, and APRMs is to demonstrate the 
    operability of the instrumentation. Therefore, 24 hours is a 
    reasonable time to permit the surveillances to be performed upon 
    entering the mode or condition in which the surveillance is 
    required.
        e. The proposal to include the performance of channel checks as 
    requirements of technical specifications is administrative in 
    nature. Presently, channel checks performed for the applicable 
    analog instrumentation in reactor vessel water level applications is 
    controlled solely by procedure. Adding this 
    [[Page 11129]] requirement to the technical specifications provides 
    for the appropriate controls of the surveillances, above and beyond 
    that presently controlled by procedure.
        f. The proposed administrative changes are offered to correct 
    typographical errors and delete cycle specific footnotes which are 
    no longer applicable. The nature of the changes precludes them from 
    impacting previously analyzed accidents.
        The proposed changes therefore do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        a. The proposed changes increase the STI and AOT for certain 
    actuation instrumentation in the RPS, ECCS, Isolation, CRBF, RCIC, 
    ATWS-RPT, EOC-RPT, Monitoring, and Feedwater/Main Turbine Trip 
    systems. There are no changes in instrumentation configuration and 
    function, and no instrumentation setpoints are changed.
        b. The changes to the Feedwater/Main Turbine Trip LCO action 
    statements allow the plant operators a maximum degree of operational 
    flexibility, while maintaining the instrumentation and protection 
    needed for terminating the feedwater controller failure transient. 
    The single failure proof criterion of the level sensors is 
    maintained, and the logic of the protective instrumentation is not 
    compromised. The changes to the LCO action statements do not 
    constitute a change to the facility or its operation as described in 
    the Safety Analysis Report.
        c. Deleting the requirement for surveilling the APRM Neutron 
    Flux--High, Setdown functional unit in Operating Condition 1 does 
    not degrade thermal margins. The margin accommodates the anticipated 
    maneuvers associated with plant power ascension. During a plant 
    shutdown, rod insertion maneuvers, recirculation flow reduction, and 
    xenon build-in all contribute to negative reactivity insertion which 
    precludes the degradation and violation of thermal margins. The 
    functions of the APRMs required to be OPERABLE in Operational 
    Condition 1 which are in effect remain to ensure that reactor core 
    thermal margins are not compromised.
        d. The conduct of neutron instrument functional tests in the 
    plant mode or condition in which the trips are applicable eliminates 
    unnecessary testing during normal plant operations. The expected 
    result of the functional testing is to demonstrate the operability 
    of the instruments. The failure of any single instrument channel 
    will neither cause nor prevent either a reactor scram or a control 
    rod block.
        e. Including the performance of channel checks for the 
    applicable analog instrumentation as part of the technical 
    specifications transfers control of the required surveillances from 
    procedure to the technical specifications, as appropriate. The 
    administrative nature of this change does not alter the functions, 
    setpoints, or configuration of the associated instrumentation.
        f. The administrative nature of the changes prevents them from 
    affecting the functions, setpoints, or configuration of the 
    associated instrumentation from being affected by the changes.
        The proposed changes do not create the possibility for an 
    accident or malfunction of a different type than any previously 
    evaluated in the UFSAR.
        (3) Involve a significant reduction in the margin of safety 
    because:
        a. Setpoints are based upon the drift occurring during an 18 
    month calibration interval. The bases in the Technical 
    Specifications either do not discuss STI, or state ``* * * one 
    channel may be inoperable for brief intervals to conduct required 
    surveillance.'' The proposed changes are bounded by the analyses of 
    the topical reports. These analyses, which were prepared by GE and 
    approved by the NRC, examined the effects of extending STI and AOT 
    and found that the proposed changes would not involve a significant 
    reduction in the margin of safety.
        b. The proposed changes to the turbine trip LCO action 
    statements do not change any of the settings of the Level 8 
    setpoints. The single failure criteria of the multiple level sensors 
    which sense and detect the Level 8 setpoint remains intact. The LCO 
    maintains the requirement that no single instrument failure will 
    prevent the feedwater pump turbines and main turbine trip on a valid 
    Level 8 signal. Scram trip signals from the turbine retain the 
    design feature that a single failure will neither initiate nor 
    impede the initiation of a reactor scram (trip).
        c. The setting, function, and conditional requirements of the 
    APRM Neutron Flux--High, Setdown function are not altered. This 
    change serves to achieve consistency between two Technical 
    Specifications Tables. This eliminates the need for surveilling a 
    function in a mode which is not applicable. The functions of the 
    APRMs required to be OPERABLE in Operational Condition 1 remain to 
    ensure that reactor core thermal margins are not compromised.
        d. The reference to 4.0.4 applicability will assist to ensure 
    consistent interpretation of the technical specifications by the 
    plant operators. This assists in ensuring that the plant is operated 
    within technical specification limitations. This change does not 
    affect trip instrumentation setpoints, and the scram function of the 
    RPS is assured by the weekly functional testing of the Manual Scram.
        e. Including the instrumentation channel checks as part of 
    technical specification requirements provides an appropriately 
    regimented method of controlling the conduct of the surveillances. 
    None of the functions, setpoints, or configuration of the associated 
    analog instrumentation is affected by this administrative change.
        f. The administrative nature of the changes serves to provide 
    more concise guidance to the plant operating staff, and as such do 
    not impact the safety margin.
        The proposed changes do not significantly reduce the margin of 
    safety as defined in the basis for any Technical Specification.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: January 13, 1995.
        Description of amendment request: The proposed amendments would 
    revise the pressure alarm setpoint allowable values for the emergency 
    core cooling system (ECCS) and reactor core isolation cooling (RCIC) 
    system ``keep filled'' pressure instrumentation channels. The purpose 
    of the proposed change is to lower the setpoint allowable values for 
    these parameters to more realistic values based upon calculations 
    performed by the licensee reflecting design changes and system 
    performance. Also, the term ``setpoint'' is being changed to ``setpoint 
    allowable value'' to clarify the use of the values. Additionally, two 
    administrative/editorial changes are included to delete technical 
    specification footnotes which are no longer applicable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Commonwealth Edison has evaluated the proposed Technical 
    Specification Amendment and determined that it does not represent a 
    significant hazards consideration. Based on the criteria for 
    defining a significant hazards consideration established in 10 CFR 
    50.92, operation of LaSalle County Station Units 1 and 2 in 
    accordance with the proposed amendment will not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        a. The proposed change in the technical specification allowable 
    values for the ECCS and RCIC discharge line ``keep filled'' alarm 
    instrument channels does not change the design bases or function of 
    these systems as described in the technical specifications and 
    UFSAR. An analysis performed by engineering demonstrates that the 
    proposed allowable values are sufficient for verifying that the ECCS 
    and RCIC pump discharge lines are full of water. In addition, 
    setpoint [[Page 11130]] calculations have been performed to verify 
    that sufficient margin exists between the recommended calibration 
    setpoints and the analytical limits for these instrument channels to 
    account for all applicable instrument errors. This provides high 
    assurance that the trip setpoints of these instrument channels will 
    not drop below the minimum required value. The ``keep filled'' 
    instrumentation is not a factor in the assumptions of any accidents, 
    thus, the probability of analyzed accidents is not increased.
        b. The proposed technical specification amendment does not 
    revise the configuration of the ECCS and RCIC discharge line ``keep 
    filled'' instrument channels or sensing lines. The proposed setpoint 
    allowable values and associated calibration setpoints are within the 
    calibration ranges of the existing pressure switches. Thus, 
    implementation of the proposed amendment does not involve any 
    physical alterations to the plant except for the recalibration of 
    the pressure switches to the new calibration setpoints.
        c. The ECCS and RCIC discharge line ``keep filled'' instrument 
    channels only perform a monitoring function. Other than ensuring 
    system readiness they do not perform a function important to safety. 
    Thus, the probability of a ECCS or RCIC failure is not increased 
    since the operation and function of the ECCS and RCIC discharge line 
    fill systems is not affected by this change.
        d. The failure of a ECCS or RCIC discharge line fill system will 
    not go undetected by the proposed change, since water leg pump trips 
    are annunciated in the control room. In addition, quarterly 
    surveillances are performed on these pumps to check for degradation.
        e. The ECCS and RCIC discharge line fill systems are not used to 
    mitigate the consequences of an accident or transient. These systems 
    are not required after the ECCS and RCIC pumps are activated.
        Therefore, the proposed change does not cause an increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because: This 
    technical specification amendment only lowers the trip setpoint 
    allowable values for the ECCS and RCIC discharge line ``keep 
    filled'' alarm instrumentation channels. As described above, the 
    proposed setpoint allowable values are sufficient for verifying that 
    the ECCS and RCIC discharge lines are full of water. Thus, the 
    probability of a water hammer occurring during system activation for 
    a surveillance test is not increased. In addition, each instrument 
    channel is independent from the other channels so that a failure in 
    one channel will not propagate to another channel. Therefore, the 
    operation of the facility in accordance with the proposed amendment 
    does not create the possibility of a new or different kind of 
    accident.
        (3) Involve a significant reduction in the margin of safety 
    because: The margin of safety is not affected by this amendment, 
    because this change involves monitoring instrumentation only. The 
    purpose of the ECCS and RCIC discharge line ``keep filled'' alarms 
    is to alert the operators when a ECCS or RCIC system may not be 
    operable due to empty or partially empty discharge lines. The 
    proposed amendment does not alter or degrade this function, since 
    the new setpoint allowable values are adequate for verifying that 
    the discharge lines are full of water. Therefore the operation of 
    the facility in accordance with the proposed amendment does not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: Robert A. Capra.
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of amendment request: January 13, 1995
        Description of amendment request: The proposed amendment would 
    modify the required settings, and allowable ``as found'' and ``as 
    left'' tolerances for the primary and secondary safety valves. The 
    proposed limits would allow installed primary and secondary valve 
    settings to be within a 3% tolerance of their nominal settings, but 
    would require returning the valve settings to within 1% of the nominal 
    settings if the valves are removed from the piping for maintenance or 
    testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The following evaluation supports the finding that operation of 
    the facility in accordance with the proposed technical specification 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to the Technical Specifications increases 
    the acceptable as found tolerance for the pressurizer safety valves. 
    The most limiting overpressure event, loss of external load, has 
    been analyzed to account for this change. The loss of external load 
    analysis was performed using a conservative 25% steam generator tube 
    plugging and an initial pressurizer level of 67.8% (providing an 
    approximate 10% conservative margin above programmed pressurizer 
    level for full power). Primary and secondary safety valve 
    accumulation was conservatively accounted for and the setpoint 
    tolerance of +3% was assumed. Reactor trip on turbine trip was 
    assumed to be disabled and the atmospheric dump valves were assumed 
    unavailable. The results of the analysis demonstrated primary and 
    secondary system pressures within 110% of design pressures. 
    Therefore, the consequences of overpressurization events will not be 
    significantly increased with a +3% tolerance on the primary safety 
    valve setpoints. The proposed Technical Specifications change will 
    not affect normal plant operation and will not increase the 
    probability of an accident.
        A review of all DNB [departure from nucleate boiling] analyses 
    was performed to ensure that predicted pressurizer pressures for 
    those analyses would not be affected by a -3% tolerance on the 
    lowest setpoint valve. The DNB analyses for which significant 
    primary system pressure increases were predicted do not result in 
    pressures high enough to lift the pressurizer safety valves with the 
    proposed tolerance. A conservative DNB analysis that bounds the 
    consequences of inadvertent opening of a pressurizer safety valve 
    has also been previously performed with predicted acceptable 
    results. If a pressurizer safety valve were to stick open, the 
    consequences would be bounded by the small break LOCA [loss-of-
    coolant accident] analysis. Therefore, the consequences due to a -3% 
    tolerance on the primary safety valve setpoints will not increase 
    the consequences or probability of an accident.
        The proposed revision removes the requirement for one operable 
    pressurizer safety valve to be installed whenever the reactor head 
    is on the vessel. Instead, proposed Specification 3.1.7.1 requires 
    all pressurizer safety valves to be operable above cold shutdown, 
    and overpressure protection during cold shutdown is provided by 
    existing Specification 3.1.8.2, Power Operated Relief Valves.
        The proposed Technical Specifications change also lists the lift 
    settings for each of the primary and secondary system safety valves. 
    This change will not affect the operation or function of the valves. 
    Therefore, the probability and consequences of previously evaluated 
    accidents will not be increased.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed changes to Technical Specifications will not affect 
    the manner in which the plant operates. The proposed increase in 
    pressurizer safety valve lift setting tolerance could change the 
    pressure at which the valves open in an overpressurization event, 
    but would not create the possibility of a new or different kind of 
    accident. Since Technical Specification 3.1.8 addresses primary 
    system overpressurization during cold shutdown, the proposed removal 
    of the requirement for an operable pressurizer safety valve to be 
    installed whenever the reactor head is on the vessel will not create 
    [[Page 11131]] the possibility of a new overpressurization event 
    during cold shutdown. The proposed change to list the lift settings 
    for the individual primary and secondary safety valves will have no 
    effect on the safety function of the valves. Therefore, the proposed 
    changes will not create the possibility of a new or different kind 
    of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to Technical Specifications do not affect 
    the DNB analyses that have been previously performed. The most 
    limiting overpressurization event, loss of external load, has been 
    conservatively analyzed accounting for the proposed changes and 
    demonstrated that the primary and secondary system pressures remain 
    within 110% of the design pressures. Overpressurization during cold 
    shutdown is addressed by Technical Specification 3.1.8. Therefore, 
    the proposed changes do not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: John N. Hannon.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan.
    
        Date of amendment request: February 10, 1995.
        Description of amendment request: The proposed amendment would 
    modify the Technical Specifications to allow a one time deferral of 
    several 18-month interval surveillance tests until the upcoming 
    scheduled refueling outage to avoid the necessity of imposing a plant 
    shutdown solely for the sake of their performance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The following evaluation supports the finding that operation of 
    the facility in accordance with the proposed Technical 
    Specifications (TS) would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Deferring surveillance testing will introduce no new operating 
    conditions, change no equipment operating procedures, and change no 
    plant systems or equipment. Therefore, operation of the facility in 
    accordance with the proposed TS would not result in a significant 
    increase in the probability of an accident previously evaluated.
        Deferring surveillance testing of snubbers and instrument 
    channels could allow minor degradations of snubber condition or 
    small changes in instrument setpoints or calibration to progress 
    some amount beyond that point which would occur with a shorter 
    surveillance interval. A review of the recent test history for the 
    subject surveillance indicates that no significant snubber 
    degradation or instrument drift was found. It is not expected that, 
    even with the proposed surveillance deferral, snubber conditions or 
    instrument settings will be found to exceed conditions allowable by 
    the Technical Specifications. Therefore, operation of the facility 
    in accordance with the proposed TS would not result in a significant 
    increase in the consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Deferring surveillance testing will introduce no new operating 
    conditions, change no equipment operating procedures, and change no 
    plant systems or equipment. Therefore, operation of the facility in 
    accordance with the proposed TS would not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        A review of past performance of the subject surveillance tests 
    indicate that the requested deferral of testing would not have a 
    significant effect on the results of the tests when they are 
    performed prior to the startup for cycle 12. Most of the affected 
    instrumentation is monitored each shift by channel checks, which 
    would disclose major failures or significant drift. Therefore, 
    operation of the facility in accordance with the proposed TS would 
    not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: John N. Hannon.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: November 2, 1994.
        Description of amendment request: The proposed amendment would 
    delete the content of the Appendix B, Environmental Protection Plan 
    (EPP) and modify License Conditions 2.C.(2) to delete that portion 
    which refers to the EPP. Specifically, the requirements for non-
    radiological environmental monitoring have been completed. The 
    radiological environmental monitoring requirements have been 
    incorporated into Appendix A (the Technical Specifications). There 
    would be no impact on the continued safety of the McGuire station by 
    deleting Appendix B.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Deletion of the Environmental Protection Plan and modifying 
    License Condition 2.C.(2) will have no impact on the probability or 
    consequences of an accident previously evaluated because the changes 
    will not have any impact upon the design or operation of any plant 
    systems or components.
        The proposed revision will not create the possibility of a new 
    or different kind of accident from any previously evaluated because 
    the revision is administrative in nature and will not change the 
    types and amounts of effluent that will be released.
        The proposed revision will not reduce a margin of safety because 
    it is administrative in nature and will not effect the margin of 
    safety as defined in the basis for any Technical Specifications.
        Accordingly, this proposed changes does not involve a 
    significant hazard.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242.
        NRC Project Director: Herbert N. Berkow. [[Page 11132]] 
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: January 18, 1995.
        Description of amendment request: The proposed amendments would 
    relocate the requirements for the seismic instrumentation, 
    meteorological instrumentation, and loose-part detection system from 
    the Technical Specifications to the Selected Licensee Commitment (SCL) 
    Manual. This will allow future changes to these controls to be 
    performed under the provisions of 10 CFR 50.59. No changes are being 
    made to the technical content of the affected Technical Specification 
    pages.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1
    
        The requested amendments will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Relocation of the affected TS sections to the SLC Manual 
    will have no effect on the probability of any accident occurring. In 
    addition, the consequences of an accident will not be impacted since 
    the above instrumentation will continue to be utilized in the same 
    manner as before. No impact on the plant response to accidents will 
    be created.
    
    Criterion 2
    
        The requested amendments will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. No new accident causal mechanisms will be created as a 
    result of relocating the affected TS requirements to the SLC Manual. 
    Plant operation will not be affected by the proposed amendments and 
    no new failure modes will be created.
    
    Criterion 3
    
        The requested amendments will not involve a significant 
    reduction in a margin of safety. No impact upon any plant safety 
    margins will be created. Relocation of the affected TS requirements 
    to the SLC Manual is consistent with the content of the Westinghouse 
    RSTS [Revised Standard Technical Specifications], as the NRC did not 
    require technical specification controls for the affected 
    instrumentation in the RSTS. The proposed amendments are consistent 
    with the NRC philosophy of encouraging utilities to propose 
    amendments that are consistent with the content of the RSTS.
        Based upon the preceding analyses, Duke Power Company concludes 
    that the requested amendments do not involve a significant hazards 
    consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242.
        NRC Project Director: Herbert N. Berkow.
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: January 18, 1995.
        Description of amendment request: The amendments would revise 
    Technical Specification Table 4.3-3 to allow the analog channel 
    operational test interval for radiation monitoring instrumentation to 
    be increased from monthly to quarterly. The proposed amendment changes 
    would be consistent with the guidance in Generic Letter 93-05, ``Line-
    Item Technical Specifications Improvements to Reduce Surveillance 
    Requirements for Testing During Power Operation.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1
    
        The requested amendments will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Decreasing the frequency of the radiation monitor analog 
    channel operational test from monthly to quarterly will have no 
    impact upon the probability or any accident, since the radiation 
    monitors are not accident initiating equipment. Analysis of the 
    previous test data * * * shows that no significant degradation of 
    performance is to be expected by the decrease in frequency. 
    Therefore, the requested amendments will have no adverse impact upon 
    the consequences of any accident.
    
    Criterion 2
    
        The requested amendments will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. As stated above, the radiation monitors are not accident 
    initiating equipment. No new failure modes can be created from an 
    accident standpoint. The plant will not be operated in a different 
    manner.
    
    Criterion 3
    
        The requested amendments will not involve a significant 
    reduction in a margin of safety. Plant safety margins will be 
    unaffected by the proposed changes. No safety equipment which is 
    taken credit for in accident analyses will be affected by the 
    requested amendments. The availability of the affected radiation 
    monitors will be increased as a result of the proposed amendments 
    because the monitors will not have to be made unavailable for 
    testing as frequently. In addition, radiation monitor operating 
    experience supports the proposed amendments. Finally, the proposed 
    amendments are consistent with the NRC position and guidance set 
    forth in NUREG-1366 and Generic Letter 93-05.
        Based upon the preceding analyses, Duke Power Company concludes 
    that the requested amendments do not involve a significant hazards 
    consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242.
        NRC Project Director: Herbert N. Berkow.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: January 20, 1995.
        Description of amendment request: The proposed amendments will 
    relocate the operability requirements for the INCORE DETECTORS (TS 3/
    4.3.3.2) to the Updated Final Safety Analysis Report, and revise Linear 
    Heat Rate surveillance 4.2.1.4, and Special Test Exceptions 
    surveillances 4.10.2.2, 4.10.4.2 (Unit 2 only), and 4.10.5.2, 
    accordingly.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes are administrative in nature in that the 
    specifications for [[Page 11133]] operation and surveillance of the 
    Incore Instrumentation (ICI) System will be relocated from the 
    Technical Specifications to the Updated Final Safety Analysis Report 
    for St. Lucie Unit 1 and Unit 2. Changes to the system will be 
    controlled by 10 CFR 50.59, and the safety analysis report is 
    required to be updated pursuant to 10 CFR 50.71(e). Relocation of 
    these requirements to the UFSAR is consistent with the NRC ``Final 
    Policy Statement on Technical Specifications Improvements for 
    Nuclear Power Reactors'' published in the Federal Register (58 FR 
    39132) dated July 22, 1993.
        Incore instrumentation is not an accident initiator nor a part 
    of the success path(s) which function to mitigate accidents 
    evaluated in the plant safety analyses. The proposed technical 
    specification change does not involve any change to the 
    configuration or method of operation of any plant equipment that is 
    used to mitigate the consequences of an accident, nor do the changes 
    alter any assumptions or conditions in any of the plant accident 
    analyses. Therefore, operation of the facility in accordance with 
    the proposed amendment would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendment to relocate the existing Technical 
    Specification requirements for the Incore Instrumentation System to 
    the Updated Final Safety Analysis Report will not change the 
    physical plant or the modes of plant operation defined in the 
    Facility License. The change does not involve the addition or 
    modification of equipment nor does it alter the design or operation 
    of plant systems. Therefore, operation of the facility in accordance 
    with the proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed changes are administrative in nature in that 
    operating and surveillance requirements for the Incore 
    Instrumentation System will be relocated from the Technical 
    Specifications to the Updated Final Safety Analysis Report for St. 
    Lucie Unit 1 and Unit 2. The ICI system is not used to actuate 
    safety-related equipment, provide interlocks, or otherwise perform 
    automatic plant control functions. The system is used to monitor 
    core power distribution parameters whose limits do involve a margin 
    of safety; however, the ICI system itself makes no contribution to 
    that margin of safety, and the power distribution limits will not be 
    changed by the proposed amendment. Therefore, operation of the 
    facility in accordance with the proposed amendment would not involve 
    a significant reduction in a margin of safety.
        Based on the above discussion and the supporting Evaluation of 
    Technical Specification changes, FPL has determined that the 
    proposed license amendment involves no significant hazards 
    consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
        Attorney for licensee: Harold F. Reis, Esquire, Newman and 
    Holtzinger, 1615 L Street, NW., Washington, DC 20036.
        NRC Project Director: David B. Matthews.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: January 17, 1995.
        Description of amendment request: The licensee proposes to revise 
    the technical specifications to reference Topical Report NF-TR-95-01 as 
    the documentation of the licensee's proficiency in performing certain 
    reload design calculations once the NRC has evaluated and approved NR-
    TR-95-01.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The addition of the reference to FPL [Florida Power and Light 
    Company] topical report which demonstrates FPL's ability to perform 
    certain reload design calculations for Turkey Point Units 3 and 4 is 
    administrative in nature and has no impact on the probability or 
    consequences of any Design Bases Event (DBE) occurrences previously 
    evaluated. The reload design calculations will be performed using 
    methodologies and computer codes approved by the NRC and poses no 
    increase in the probability or consequences of any accident 
    previously evaluated.
        The Core Operating Limits Report (COLR) parameters will be 
    evaluated every cycle to ensure proper compliance with the Updated 
    Final Safety Analysis Report (UFSAR). These limits will be evaluated 
    in accordance with 10 CFR [Section] 50.59, which ensures that the 
    reload will not involve an increase in the probability of 
    occurrences or consequences of an accident previously evaluated. 
    Title 10 CFR [Section] 50.59 (2) states that a proposed change 
    involves an unreviewed safety question (i) if the probability of 
    occurrence or the consequences of an accident or malfunction of 
    equipment important to safety previously evaluated in the safety 
    analysis report may be increased. Consequently, since any change to 
    the reload core design analysis must be evaluated relative to the 
    more restrictive evaluation criterion of 10 CFR [Section] 50.59, 
    then operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The addition of the reference to FPL topical report which 
    demonstrates FPL's ability to perform certain reload design 
    calculations for Turkey Point Units 3 and 4 is administrative in 
    nature and has no impact, nor does it contribute in any way to the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. No new accident scenarios, failure mechanisms 
    or limiting single failure events are introduced as a result of the 
    proposed change.
        The generation of the Axial Flux Difference, Rod Bank Insertion 
    limits and K(Z) curve will be performed using NRC-approved 
    methodology and are submitted to the NRC, as a revision to the COLR, 
    to allow the NRC staff to trend. The Technical Specifications will 
    continue to require operation within the core operating limits and 
    appropriate actions will be taken if these limits are exceeded.
        Title 10 CFR [Section] 50.59 permits a licensee to make changes 
    in the facility as described in the safety analysis report without 
    prior Commission approval, provided that the proposed changes does 
    not involve an unreviewed safety question. 10 CFR [Section] 50.59 
    (2) states that a proposed change involves an unreviewed safety 
    question (ii) if a possibility for an accident or malfunction of a 
    different type than any evaluated previously in the safety analysis 
    report may be created. Consequently, since any change to the reload 
    core design analysis must be evaluated relative to the more 
    restrictive evaluation criterion of 10 CFR [Section] 50.59, then 
    operation of the facility in accordance with the proposed amendments 
    would not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The margin of safety is not affected by FPL performing the 
    reload design calculations for Turkey Point Units 3 and 4. The 
    supporting Technical Specification values are defined by the 
    accident analyses which are performed to conservatively bound the 
    operating conditions defined by the Technical Specifications. The 
    development of the limits for future reloads will continue to 
    conform to the methodology described in NRC approved documentation. 
    In addition, each future reload will involve a 10 CFR [Section] 
    50.59 [[Page 11134]] review to assure that operation of the units 
    within the cycle specific limits will not involve a reduction in a 
    margin of safety. 10 CFR [Section] 50.59 (2) states that a proposed 
    change involves an unreviewed safety question (iii) if the margin of 
    safety as defined in the basis for any technical specification is 
    reduced. Consequently, since any change to the reload core design 
    analysis must be evaluated relative to the more restrictive 
    evaluation criterion of 10 CFR [Section] 50.59, then operation of 
    the facility in accordance with the proposed amendments would not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration. The 
    NRC staff, however, considers that the licensee's statements relative 
    to 10 CFR Section 50.59 evaluations to be performed in the future are 
    not relevant to the proposed no significant hazards determination.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
        Attorney for licensee: Harold F. Reis, Esquire, Newman and Holtzer, 
    P.C., 1615 L Street, NW., Washington, DC 20036.
        NRC Project Director: David B. Matthews.
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of amendment request: October 28, 1994.
        Description of amendment request: The proposed amendment revises 
    the Duane Arnold Energy Center (DAEC) Operating License by deleting a 
    condition of the license that requires a ``Plan for Integrating 
    Scheduling of Plant Modifications for the Duane Arnold Energy Center'' 
    (the Plan).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is provided below:
    
        (1) The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. No physical changes to the facility will occur 
    as a result of this amendment. Work activities will continue to 
    receive the appropriate level of review in accordance with DAEC 
    procedures and practices. The organizational structure that controls 
    and manages these activities remains unchanged and will assure that 
    activities are prioritized and performed in a manner consistent with 
    plant safety. The proposed amendment removes an administrative 
    burden that is no longer required.
        (2) The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. No changes to the physical design and/or operation of the 
    plant will occur as a result of this amendment. The processes by 
    which activities are planned, prioritized, and controlled are not 
    affected. The appropriate level of technical review and management 
    oversight continue to be performed in accordance with existing 
    procedures and practices to assure that activities are performed in 
    a manner consistent with plant safety.
        (3) The proposed amendment does not involve a significant 
    reduction in a margin of safety. As stated earlier, no changes to 
    the physical design and/or operation of any plant systems will occur 
    as a result of this amendment. Work activities will continue to 
    receive the appropriate technical review and management oversight to 
    assure that activities are prioritized and performed in a manner 
    consistent with plant safety. The amendment removes an 
    administrative burden that is no longer required.
        Based on the above, we have determined that the proposed 
    amendment will not involve a significant hazards consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401.
        Attorney for licensee: Jack Newman, Kathleen H. Shea, Morgan, Lewis 
    & Bouckins, 1800 M Street NW., Washington, DC 20036.
        NRC Project Director: Leif J. Norrholm.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: January 24, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 3.4.1, ``Leakage Rate,'' to reduce the 
    allowable leakage rate of the reactor building from 2000 cubic feet per 
    minute (cfm) to 1600 cfm.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Secondary containment and RBEVS [Reactor Building Emergency 
    Ventilation System] are not initiators or precursors to an accident. 
    Secondary containment provides a pressure boundary, with limited in-
    leakage, for the purpose of preventing a ground level unfiltered 
    release of radioactivity. RBEVS responds to accidents involving 
    release of radioactivity to the secondary containment by maintaining 
    a negative pressure inside secondary containment and by providing an 
    elevated release. Therefore, a change to the Reactor Building 
    leakage rate cannot affect the probability of an accident previously 
    evaluated.
        Although the proposed change reduces the Reactor Building 
    leakage rate from 2000 cfm to 1600 cfm consistent with system 
    design, there is no effect on the radiological consequences of any 
    previously analyzed accident since the radiological analysis does 
    not assume exfiltration. Therefore, the Technical Specification 
    change does not significantly increase the consequences of a 
    previously evaluated accident.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change to the Reactor Building leakage rate from 
    2000 cfm to 1600 cfm does not involve any accident precursors or 
    initiators. During an accident involving a release of radioactivity 
    to the secondary containment, the RBEVS would be operable and 
    provide filtration of containment atmosphere prior to release to the 
    environment. This change does not involve any physical modifications 
    to the system, thus the system will operate as designed. Therefore, 
    the proposed Technical Specification change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed change in Reactor Building in-leakage from 2000 cfm 
    to 1600 cfm in Specification 3.4.1 and the associated basis is to be 
    consistent with system design and reflect the leakage rate 
    associated with approximately one building air volume change per 
    day. The resulting accident analysis remains unchanged since the 
    radiological analysis does not assume any exfiltration. Therefore, 
    the proposed change will not involve a significant reduction in the 
    margin of safety as defined in the basis for any Technical 
    Specification.
        Therefore, as determined by the above analysis, this proposed 
    amendment involves no significant hazards consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request [[Page 11135]] involves no significant hazards 
    consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Ledyard B. Marsh.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: February 1, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3.6.13, ``Remote Shutdown Panels.'' 
    TS 3.6.13 currently requires that if the valve controls or monitoring 
    instrumentation on the Remote Shutdown Panels are inoperable, they must 
    be restored to an operable status within 24 hours or the plant shall be 
    shut down. The proposed change would require inoperable valve control 
    functions be restored to an operable status within 30 days or the plant 
    shall be shut down. The proposed change would also specify that 
    required inoperable monitoring instrumentation functions be restored to 
    an operable status within 30 days or that an alternate method of 
    monitoring the parameter be established within 30 days and the required 
    function be restored to an operable status within 90 days or the plant 
    shall be shut down.
        The proposed amendment would also make minor editorial changes to 
    TS Table 3.6.13-1 so that the table entries would be consistent with 
    the proposed revisions to TS 3.6.13.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The remote shutdown panel monitoring instruments and controls 
    are not initiators or precursors to an accident. The remote shutdown 
    panels provide the operator with sufficient monitoring instruments 
    and controls to place and maintain the plant in a safe shutdown 
    condition from a location other than the control room. Therefore, 
    the proposed changes to Specification 3.6.13, ``Remote Shutdown 
    Panels,'' cannot affect the probability of a previously evaluated 
    accident.
        The proposed changes, in part, require that one channel (on 
    either panel) for each function be operable. This change could 
    potentially avoid an unnecessary plant shutdown without affecting an 
    operator's ability to cope with a control room evacuation. One 
    channel of each function is adequate to assure a safe shutdown. The 
    proposed changes would also allow 30 days to restore an inoperable 
    function to an operable status. As indicated in the ITS [Improved 
    Standard Technical Specifications], the allowed time of 30 days is 
    acceptable based on operating experience and the low probability of 
    an event that would require evacuation of the control room. With one 
    or more monitoring instrument functions inoperable, the proposed 
    change gives an operator an additional option. Specifically, the 
    operator is allowed 30 days to establish an alternate method of 
    monitoring the parameter and 90 days to restore the function to 
    operable status. The use of an alternate method is acceptable since 
    it will provide the operator with indication of the parameter of 
    interest. The remote shutdown panels will not be required to be 
    operable in hot shutdown because the plant is already subcritical 
    and in a condition of reduced reactor coolant inventory energy. 
    Because this Specification no longer applies to hot shutdown and to 
    be consistent with the guidance provided in the ITS, Specification 
    3.6.13.d will require that the plant be brought to a hot shutdown 
    condition (versus cold shutdown condition) in 12 hours. As indicated 
    in the ITS, the 12-hour completion time is reasonable based on 
    operating experience. The Bases Section to 3.6.13 and 4.6.13 was 
    revised to be consistent with the proposed changes to the 
    Specification. The Bases currently indicates that one remote 
    shutdown panel is required to be operable. As explained above, one 
    channel of each required function is required to maintain remote 
    shutdown operability. In summary, the proposed changes will not 
    affect the ability of the Remote Shutdown System to provide the 
    operator with sufficient instrumentation and controls to place and 
    maintain the plant in a safe shutdown condition from a location 
    other than the control room. Therefore, the consequences of an event 
    requiring a control room evacuation will not significantly increase.
        Editorial changes were made to Table 3.6.13-1 to be consistent 
    with the changes made to the Specification. Specifically, the word 
    ``INSTRUMENT'' was changed to ``FUNCTION'' and the words ``PANEL 
    MONITORING'' were changed to the words ``PANELS FUNCTIONS.'' These 
    changes make it clear that one channel of each function, on either 
    panel is acceptable to maintain operability. The emergency condenser 
    condensate return valve control and motor-operated steam supply 
    valves control were relocated from Specification 3.6.13.b to Table 
    3.6.13-1 to be consistent with the proposed changes.
        Based on the above, the consequences of an accident previously 
    evaluated are not significantly increased.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The changes do not introduce any new accident precursors and do 
    not involve any alterations to plant configurations which could 
    initiate a new or different kind of accident. The proposed changes 
    require that one channel of each function be operable to assure the 
    remote shutdown panels can meet their intended function. No changes 
    have been made which will affect the operation of the remote 
    shutdown panels in a way which would create a new or different kind 
    of accident. Therefore, the proposed changes will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed changes will not affect the ability of the Remote 
    Shutdown System to provide the operator with sufficient 
    instrumentation and controls to place and maintain the plant in a 
    safe shutdown condition from a location other than the control room. 
    The ability to respond to a control room evacuation is maintained 
    with one channel operable for each required function. The allowed 
    outage time of 30 days is acceptable based on operating experience 
    and the low probability of an event requiring control room 
    evacuation. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Ledyard B. Marsh.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: January 10, 1995.
        Description of amendment request: The proposed amendment request 
    would revise Technical Specifications by deleting the power range, 
    neutron flux, high negative rate trip from Tables 2.2-1, 3.3-1, and 
    4.3-1, and delete the associated Bases Section 2.0. [[Page 11136]] 
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
    * * * The proposed changes would not involve an SHC because the 
    changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The deletion of the power range, neutron flux, high negative 
    rate trip will not adversely affect plant operations. As has been 
    presented and accepted by the NRC Staff in previous docketed 
    correspondence, the dropped RCCA [rod cluster control assembly] 
    accident analysis does not rely on this trip to safely shut down the 
    plant. The safety analysis of the plant is unaffected by the 
    proposed changes. Since the safety analysis is unaffected, the 
    calculated radiologicalreleases associated with the analysis are not 
    affected. Therefore, the proposed changes will not increase the 
    probability or consequences of an accident previously evaluated.
        The reactor trip system is used to mitigate accidents. There 
    have been instances, during calibration of these units, where a 
    single channel has generated a trip signal. Leaving this in place 
    when it is not necessary could, therefore, cause a reactor trip. The 
    deletion of one trip function will, therefore, slightly decease, not 
    increase, this probability.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The reactor trip system is used to mitigate accidents, and the 
    only way that it can initiate an event is by causing the reactor to 
    trip when it is unnecessary. This possibility of the generation of a 
    false trip signal has already been evaluated in the safety analysis. 
    This modification will physically remove or disable the power range, 
    neutron flux trip and will therefore decrease the possibility for 
    the generation of a false trip signal. Therefore, the proposed 
    change cannot create a new or different kind of accident from any 
    previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change which deletes the power range, neutron flux, 
    high negative rate trip will have no impact on the margin of safety. 
    The current safety analysis for Millstone Unit No. 3 does not credit 
    this trip for any events; therefore, removal of this trip from the 
    technical specifications will not affect the margin of safety for 
    any analyzed events.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: January 23, 1995.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) by 1) adding a new Section 3/
    4.5.5 which provides a limiting condition for operation, an action 
    statement, a surveillance requirement, and a corresponding bases 
    section, for the trisodium phosphate (TSP) baskets which will be 
    installed in the next refueling outage; 2) deleting Section 3/4.6.2.3 
    and Bases 3/4.6.2.3 related to the spray additive system which are no 
    longer needed since the chemical addition tank is being abandoned; and 
    3) updating Index Pages viii, ix, and xiv to reflect the above changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
     * * * The proposed changes do not involve an SHC because the 
    changes would not:
        1. Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        The plant change affects the chemical composition of the QSS 
    [quench spray system] flow and the method of sump pH control, which 
    are important for containment heat removal/pressure mitigation (MSLB 
    and LOCA) [main steamline break and loss-of coolant accident] and 
    fission product removal (LOCA). However, this change does not affect 
    the probability of occurrence of these accidents. Since the TSP 
    baskets are passive devices located inside the containment, they 
    cannot initiate a transient or affect the probability of occurrence 
    of any previously evaluated accident.
        The design change will not adversely affect the radiological 
    doses for the DBA [design basis accident] LOCA at the Exclusion Area 
    Boundary, Low Population Zone, Millstone Unit No. 3 Control Room, 
    Millstone Unit No. 2 Control Room, and the Millstone Technical 
    Support Center. Also, the change will not adversely affect the 
    calculated peak clad temperature (PCT) for the DBA LOCA.
        2. Create the Possibility of a New or Different Kind of Accident 
    from any Previously Analyzed.
        The change does not create a malfunction that is different from 
    those previously evaluated. The TSP baskets are passive devices that 
    have minimal impact on any other systems except through water 
    chemistry. The change in water chemistry does not adversely affect 
    any safety systems. The installation of the TSP baskets and the 
    abandonment of the CAT [chemical addition tank] will not change the 
    probability of a malfunction of safety-related equipment.
        Potential malfunctions relating to the TSP powder, the 12 
    baskets which hold the TSP powder, the QSS and other systems, and 
    equipment credited in the safety analysis were evaluated and 
    determined not to be adversely affected by the change. Additionally, 
    the transient pH behavior of the spray flow will not adversely 
    affect metals, coatings and elastomers in the containment, and the 
    performance of associated safety functions is not affected.
        Finally, the change in the chemical composition of the QSS 
    solution will not affect the operability of this system or its 
    ability for containment heat removal and pressure mitigation.
        3. Involve a Significant Reduction in the Margin of Safety.
        The design changes do not adversely affect the ability of the 
    QSS to perform the function of containment heat removal, pressure 
    mitigation and fission product (iodine) retention. The design 
    changes do not adversely affect any equipment credited in the safety 
    analysis. Also, the design changes to not increase the calculated 
    peak clad temperature (PCT) or the offsite doses due to the design 
    basis LOCA. Therefore, there is no impact on the margin of safety as 
    specified in the technical specifications.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: January 24, 1995. [[Page 11137]] 
        Description of amendment request: The amendment request would 
    revise the Technical Specification Section 3.2.3.1.a and Table 2.2-1 to 
    decrease the acceptance criterion for measured reactor coolant system 
    (RCS) flow rate from 387,480 gallons per minute (gpm) to 371,920 gpm.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
    
     * * * The proposed changes do not involve an SHC because the 
    changes would not:
        1. Involve a Significant Increase in the Probability or 
    Consequence of an Accident Previously Evaluated.
        An evaluation of the 4% decrease in the RCS total flow rate 
    limit has shown that the change does not significantly impact the 
    design basis analyses. Therefore, the change will not increase the 
    consequences of an accident previously evaluated.
        There are no actual plant changes that will result from this 
    technical specification change. Instead, the technical specification 
    requirement for minimum total RCS flow rate is being changed to 
    provide operational benefit without compromising safety. Since there 
    are no plant changes, there is no effect on the probability of 
    occurrence of previously evaluated accidents.
        The change will have a negligible impact on the small break loss 
    of coolant accident (LOCA) and large break LOCA analyses. The PCT 
    [peak cladding temperature] acceptance criteria will continue to be 
    met with the assumption of a 4% reduction in RCS flow rate.
        For the steam generator tube rupture event, both the FSAR [Final 
    Safety Analysis Report] offsite dose analysis and the margin of 
    steam generator (SG) overfill were evaluated. It was determined that 
    the 4% reduction in RCS flow rate will not adversely affect the 
    offsite doses or the margin to SG overfill and, therefore, the FSAR 
    conclusions remain unchanged.
        In the evaluation of non-LOCA transients, the DNB [departure 
    from nucleate boiling] is the most affected parameter due to a 
    change in flow rate. It was concluded that the 4% reduction in RCS 
    flow was acceptable and there was margin to the DNB limit.
        It is concluded that there is sufficient margin to the system 
    pressure, PCT and DNB limits to offset the effect of the 4% flow 
    rate decrease and the calculated radiological releases associated 
    with the analysis are not affected. Therefore, there is no effect on 
    the consequences of previously evaluated accidents.
        2. Create the Possibility of a New or Different Kind of Accident 
    from any Previously Analyzed.
        The low loop flow trip setpoint specified in Technical 
    Specification Table 2.2-1 is set as a fraction of total flow. The 
    flow fraction is not being changed and no hardware changes are 
    required due to the reduction in minimum flow. Also, the reduction 
    in minimum flow will not change the operation of any plant equipment 
    and it does not modify plant operation.
        Therefore, the reduction in minimum flow does not introduce any 
    new failure modes or malfunctions and it does not create the 
    potential for a new unanalyzed accident.
        3. Involve a Significant Reduction in the Margin of Safety.
        The proposed 4% decrease in the technical specification limit 
    for total RCS flow rate will not adversely affect the results of the 
    FSAR accident analysis, and it is concluded that this change is 
    safe. The change does not adversely affect any equipment credited in 
    the safety analysis, and it does not affect the probability of 
    occurrence of any plant accident. Also, the change has a negligible 
    impact on the PCT, and it does not increase the offsite doses or 
    decrease the DNB below its acceptance limit.
        Therefore, the change does not have any significant impact on 
    the protective boundaries, and there is no reduction in the margin 
    of safety as specified in the technical specifications.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: January 9, 1995.
        Description of amendment request: The proposed amendment to the 
    technical specifications (TSs) would delete requirements for the toxic 
    gas monitoring system (TGMS) as contained in TS 2.22 and TS 3.1, Table 
    3-3, item 29.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The previously evaluated accidents affected by this change are 
    the on-site and off-site toxic chemical releases. These events have 
    been re-evaluated for this proposed change and have been shown to 
    meet the applicable regulatory screening criteria. The deterministic 
    analyses performed show that the guidelines of Regulatory Guide 1.78 
    for control room habitability are met for on-site and most off-site 
    chemicals. On-site chemical sources originally present when the 
    toxic gas monitoring system was installed have been removed from 
    site or determined not to exceed the deterministic analysis 
    screening requirements. For those off-site chemical releases which 
    did not meet the deterministic screening criteria a probabilistic 
    analysis was performed. The probabilistic analysis performed in 
    support of this proposed change shows that the probability of an 
    off-site chemical release leading to 10 CFR 100 consequences is 
    orders of magnitude less than the SRP [Standard Review Plan] 2.2.3 
    guidelines. These results show that there is no significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        (2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        Only events involving chemicals for which the TGMS provides an 
    automatic detection/isolation function are affected by this change. 
    As stated above, the potential events involving these chemicals have 
    been re-evaluated using the appropriate regulatory guidance and 
    shown to satisfy either the deterministic screening criteria of RG 
    [Regulatory Guide] 1.78, or to be probabilistically insignificant 
    compared to the guidelines of SRP Section 2.2.3. These results show 
    that the proposed change will not create the possibility of a new or 
    different kind of accident from any previously evaluated. Therefore, 
    the proposed change does not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        (3) The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The margin of safety is defined by the regulatory basis for the 
    existing TGMS, namely NUREG-0737, Item III.D.3.4. The analysis 
    provided to support this proposed change follows the regulatory 
    guidelines of RG 1.78 and SRP Section 2.2.3, as specified in NUREG-
    0737, Item III.D.3.4. The analysis shows that the applicable 
    regulatory criteria are met and the proposed changes do not involve 
    a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: LeBoeuf, Lamb, Leiby, and MacRae, 1875 
    Connecticut [[Page 11138]] Avenue, NW., Washington, DC 20009-5728.
        NRC Project Director: Theodore R. Quay.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of amendment requests: February 6, 1995 (Reference LAR 95-01).
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant, Unit Nos. 1 and 2, to change TS 3/4.9.14.1, ``Spent Fuel 
    Assembly Storage,'' TS 3/4.9.14.2, ``Spent Fuel Pool Boron 
    Concentration,'' TS 5.3.1, ``Reactor Core--Fuel Assemblies,'' and TS 
    5.6.1, ``Fuel Storage--Criticality,'' and add new TS 3/4.9.14.3, 
    ``Spent Fuel Assembly Storage--Spent Fuel Pool Region 1.'' The specific 
    TS changes proposed are as follows:
        (1) The proposed changes to TS 3/4.9.14 are:
        (a) TS 3.9.14.1 and Figure 3.9-2 would be revised to allow the 
    storage of spent fuel assemblies with initial enrichments up to 5.0 
    weight percent uranium-235 (U-235) in Region 2 of the spent fuel pool 
    (SFP). Fuel pellet diameter would be considered in combination with 
    initial enrichment and cumulative burnup.
        (b) Editorial corrections to the titles of TS 3/4.9.14.1 and 3/
    4.9.14.2 would be made for consistency with the TS format.
        (2) New TS 3/4.9.14.3 would be added. The new TS would include:
        (a) Requirements for acceptable fuel storage in Region 1 of the 
    SFP.
        (b) An action statement, similar to that for TS 3.9.14.1, requiring 
    suspension of all fuel movement and crane operations except to move the 
    noncomplying fuel assemblies into an acceptable pattern. The action 
    statement also requires verification of SFP boron concentration at 
    least once per 8 hours.
        (c) A requirement, similar to that for TS 4.9.14.1, for an 
    evaluation that considers enrichment, boron content, and cumulative 
    burnup of each fuel assembly before storage in Region 1 of the SFP.
        (d) New Figure 3.9-3 for use in determining the acceptability of 
    storing fuel in Region 1 of the SFP.
        (3) The proposed changes to TS 5.3.1 are:
        (a) The number of fuel rods in each fuel assembly, nominal length 
    of each fuel rod, and maximum fuel enrichment would be removed.
        (b) The current allowance for fuel rod substitutions as justified 
    by analysis would be clarified to specify that the analysis be 
    performed using NRC staff-approved methods.
        (c) An allowance to use a limited number of lead test assemblies in 
    nonlimiting core locations would be added.
        (d) The current specification requiring Zircaloy-4 fuel cladding 
    would be changed to allow Zircaloy-4 or ZIRLO cladding.
        (4) The proposed changes to TS 5.6 are:
        (a) TS 5.6.1.1 would be renumbered TS 5.6.1 and the word 
    ``borated'' would be replaced with ``unborated.''
        (b) A new requirement would be added to specify the maximum fuel 
    enrichment allowed to be stored in the fuel racks.
        (c) TS 5.6.1.2 would be deleted.
        (5) The associated Bases would also be appropriately revised.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Analyses were performed to verify that an increase in enrichment 
    of the fuel from 4.5 weight percent U-235 to 5.0 weight percent U-
    235 would not result in an inadvertent criticality event in the new 
    fuel storage racks or the SFP. The analyses indicate that for the 
    new fuel racks, the keff will remain below 0.95 if flooded with 
    non-borated water, and below 0.98 if flooded with optimum-density 
    aqueous foam. The analyses indicate that for the spent fuel racks, 
    assuming credit for soluble boron in accident scenarios, the 
    keff will remain below 0.95 as required.
        The increase in the fuel enrichment from 4.5 weight percent U-
    235 to 5.0 weight percent U-235 does not change any of the external 
    dimensional characteristics of the fuel element, the fuel storage 
    racks, or the SFP itself. The accidents originally evaluated 
    considered those events that could lead to fuel damage and release 
    of radioactive material primarily from mechanical means, such as 
    physical impact on the fuel or the SFP. Because the physical design 
    and methods of operation are the same as previously evaluated, there 
    is no change in the probability of occurrence of such events.
        The maximum spent fuel gap activity and the resulting offsite 
    dose consequences after a postulated fuel handling accident are 
    primarily dependent on fuel burnup, and are not significantly 
    affected by an increase in fuel enrichment. For up to 5.0 weight 
    percent U-235 and 60,000 MWD/MTU burnup, NUREG/CR-5009 indicates 
    that fuel handling accident offsite doses could increase by a factor 
    of 1.2, which indicates that doses would still remain within 10 CFR 
    Part 100 limits.
        The Generic Letter 90-02 Supplement 1 change to TS 5.3.1 
    clarifies the requirements associated with fuel reconstitution. It 
    does not change the methodology that would be used to reconstitute 
    fuel.
        The use of ZIRLO cladding will not increase the probability or 
    consequences of an accident, since it has improved mechanical 
    properties such as a lower corrosion rate and reduced radiation-
    induced growth.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The physical and mechanical parameters associated with the fuel 
    assemblies and spent fuel racks are the same as previously 
    evaluated. Therefore, any malfunctions related to the physical 
    aspects of fuel storage are the same as previously evaluated.
        The conditions for fuel storage in the proposed new TS 3.9.14.3 
    provide new criteria for locations where a fuel assembly could be 
    incorrectly placed. However, the incorrect placement of a fuel 
    assembly has been analyzed, and would not cause an inadvertent 
    criticality or any other accident.
        The change to 5.0 weight percent U-235 does not result in 
    physical alterations or changes to the operation of the plant, or 
    change the method by which any safety-related system performs its 
    function. The use of ZIRLO cladding does not result in a significant 
    change to the plant.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The acceptance criteria of a keff of 0.95 (or 0.98 for the 
    new fuel rack optimum moderation accident) provides the margin to 
    criticality. Analyses were performed that conclude that the proposed 
    changes to allow up to 5.0 weight percent U-235 in the new and spent 
    fuel racks meet the acceptance criteria. The use of ZIRLO cladding 
    will not reduce the protection of the public health or safety, as 
    indicated in the NRC's revisions to 10 CFR 50.44 and 50.46 (57 FR 
    39355).
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    [[Page 11139]] Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: Theodore R. Quay.
    
    Pacific Gas and Electric Company, Docket No. 50-133, Humboldt Bay Power 
    Plant, Unit 3, Humboldt County, California
    
        Date of amendment request: November 23, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications Section VI, ``Waste Disposal 
    Systems,'' regarding radioactive effluent limitations and the 
    conditions for automatically pumping the contents of the reactor 
    caisson sump to the outfall canal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed revisions to the HBPP Technical Specifications 
    remove the ambiguity in the guidelines for directing caisson sump 
    discharges to the outfall canal. Additionally, the proposed 
    revisions will modify Section VI to be consistent with the guidance 
    provided by NRC Draft Generic Letter for 10 CFR 20 Modification to 
    Technical Specifications (58 FR 68171, dated December 23, 1993). 
    These changes in effluent limits are not related to the probability 
    or consequences of an accident.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed revisions to the HBPP Technical Specifications are 
    administrative in nature and do not change the method by which any 
    safety-related system performs its function.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed revisions to the HBPP Technical Specifications do 
    not affect the margin of safety associated with parameters for any 
    accident analysis.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Humboldt County Library, 636 F 
    Street, Eureka, California 95501.
        Attorney for licensee: Christopher J. Warner, Esquire, Pacific Gas 
    & Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: Seymour H. Weiss.
    
    Pacific Gas and Electric Company, Docket No. 50-133, Humboldt Bay Power 
    Plant, Unit 3, Humboldt County, California
    
        Date of amendment request: November 23, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications Section VII.C, Plant Staff, to 
    decrease the minimum staff requirements for the shift operating 
    organization from five to two persons.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The probability or consequences of an accident previously 
    evaluated will not be affected by the change in plant staffing. The 
    plant staff manning requirements for the shift operating 
    organization are being reduced to reflect the condition of the plant 
    in a SAFSTOR mode. Previously evaluated accidents do not require 
    operator actions to mitigate or reduce the consequences of 
    occurrence. Consequently, the change will not affect the probability 
    or consequences of an accident occurring.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed revisions to the HBPP Technical Specifications are 
    administrative in nature. Further, there would not be any change in 
    equipment or system function or operation.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed revisions to the HBPP Technical Specifications do 
    not affect the margin of safety of any accident analysis since they 
    do not affect the parameters for any accident analysis, and they 
    have no effect on the current operating methodologies or actions 
    that govern plant performance.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Humboldt County Library, 636 F 
    Street, Eureka, California 95501.
        Attorney for licensee: Christopher J. Warner, Esquire, Pacific Gas 
    & Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: Seymour H. Weiss.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket No. 
    50-278, Peach Bottom Atomic Power Station, Unit No. 3, York County, 
    Pennsylvania
    
        Date of application for amendment: January 13, 1995.
        Description of amendment request: The proposed changes revise 
    Tables 3.7.1 and 3.7.4 to reflect a reduction in the number of primary 
    containment power operated outboard valves for the Traversing Incore 
    Probe (TIP) probes, and a redesignation of the containment penetration 
    numbers for the TIP ball, shear, and check valves. The proposed changes 
    are a result of PBAPS Modification P00068.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The TIP system does not serve as an initiator or contributor to 
    any accidents previously evaluated. The system provides a means of 
    calibrating the Local Power Range Monitors and supports thermal 
    limit calculations. The new system performs the same function as the 
    old one. It will provide improved reliability and added redundancy 
    by allowing a complete flux mapping if a detector or drive failure 
    were to occur.
        Installation of Modification P00068 and its operation will not 
    degrade any active or passive equipment that responds to an 
    accident. These changes do not decrease the 
    [[Page 11140]] effectiveness of equipment relied upon to mitigate 
    the previously evaluated accidents.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The modification is considered an enhancement to the TIP system 
    and does not serve as an initiator or contributor to any of the 
    accidents previously evaluated. The proposed changes do not 
    introduce a new mode of plant operation. The new system, like the 
    old one, is designed to keep the ball valves closed upon reset of 
    the Primary Containment Isolation System (PCIS) logic. The new TIP 
    control console will respond to a PCIS isolation signal in the same 
    manner as the old system.
        Implementation of the proposed changes will not affect the 
    design function or configuration of any component or introduce any 
    new operating scenarios or failure modes or accident initiation.
        Modification P00068 will not impair or prevent safety systems 
    from performing their safety function. It will not make any changes 
    to the design function of the TIP system. The classification of the 
    TIP ball and shear valves and their control circuitry will not 
    change as a result of this modification.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The TIP system does not serve as an initiator or contributor to 
    any accidents evaluated in the SAR [safety analysis report]. 
    Modification P00068 is considered an enhancement to the existing TIP 
    system and does not change its design function. The reduction in the 
    number of containment penetrations from five to three does not 
    represent a reduction in a margin of safety because of additional 
    indexers in the new system. The proposed changes do not adversely 
    affect the assumptions or sequence of events used in any accident 
    analysis.
        Therefore, the proposed changes do not involve a reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for Licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    Pennsylvania 19101.
        NRC Project Director: John F. Stolz.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: June 13, 1994.
        Description of amendment request: The proposed change would remove 
    license condition 2.E from the Facility Operating License. License 
    Condition 2.E incorporated the requirements of U.S. Department of 
    Interior publication ``Environmental Criteria for Electric Transmission 
    Systems''--1970, which applies to the construction cleanup, 
    restoration, and maintenance of transmission lines.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
        (1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change will remove a license condition unrelated to 
    nuclear safety. License condition 2.E incorporated into the 
    Operating License the requirements of U.S. Department of Interior 
    publication ``Environmental Criteria for Electric Transmission 
    Systems''--1970. The goal of this standard is to ``safeguard 
    aesthetic and environmental values within the constraints imposed by 
    the current state of high-voltage transmission technology.'' License 
    condition 2.E addresses the preservation of the environment and 
    natural resources. Removing this condition from the Facility 
    Operating License has no bearing on plant safety or the health and 
    safety of the public considering its non-nuclear nature. The 
    transmission line right-of-ways maintained by the [Power] Authority 
    [of the State of New York] are subject to regulation by other State 
    and Federal Agencies. Removal of this license condition will not 
    affect operation of safety related structures, systems or components 
    nor affect the quality assurance program at the FitzPatrick plant. 
    Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        (2) create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        License condition 2.E of the James A. FitzPatrick Plant 
    Operating License applies to the construction cleanup, restoration, 
    and maintenance of transmission lines. The Authority's transmission 
    lines are managed under guidelines based on the ``Generic 
    Transmission Line Right-of-Way Management'' plan requirements. The 
    requirements imposed by the plan on the FitzPatrick transmission 
    line right-of-ways exceed those of the U.S. Department of Interior 
    publication referenced in license condition 2.E in both scope and 
    details. Therefore, implementing the proposed change will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        (3) involve a significant reduction in a margin of safety.
    
        License condition 2.E of the James A. FitzPatrick Plant 
    Operating License applies to the construction cleanup, restoration, 
    and maintenance of transmission lines. The requirements imposed by 
    this license condition are unrelated to nuclear safety. Continued 
    operation of the plant without Condition 2.E does not involve a 
    significant reduction in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Ledyard B. Marsh.
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: December 16, 1994; supplemented February 
    10, 1995 (TS 94-07).
        Description of amendment request: The proposed change would reduce 
    the maximum allowed power levels and more clearly specify the plant 
    conditions allowed by the technical specifications for operation with 
    one or more main steam safety valves inoperable. In addition, the Bases 
    would be revised to reflect these changes and incorporate the revised 
    methodology used to establish the neutron flux setpoints.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of [[Page 11141]] Sequoyah Nuclear Plant (SQN) 
    in accordance with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        This change reduces the power level at which the reactor may be 
    operated with one or more main steam safety valves (MSSVs) 
    inoperable, to ensure that the secondary system is not 
    overpressurized during the most severe pressurization transient of 
    the secondary side. Additionally, this change will combine the TS 
    action statements for 3- and 4-loop operation with one or more MSSVs 
    inoperable, revise the mode requirements and times of Action 
    Statement 3.7.1.1.a, and correct a reference in the bases section to 
    Table 3.7-1. Reduction of the high neutron flux (HNF) trip setpoint 
    will continue to be used as the means to ensure that the required 
    reactor power level reductions are met. Mode 3 will be limited to 
    application when the reactor trip breakers (RTB) are closed. Lack of 
    NIS trip setpoint adjustments with the RTB open has no effect on the 
    accident analysis. There is no change to the function of the MSSVs 
    by the proposed change. This change will not alter any accident 
    analysis assumptions or results for SQN. The proposed change will 
    reduce the amount of relief capacity required to mitigate the 
    consequences of the transient by reducing the total amount of energy 
    in the primary system. Therefore, this change will not increase the 
    probability of an accident.
        This change is consistent with current SQN accident analysis 
    assumptions for the MSSVs and does not change the containment 
    response for any design basis event. Therefore, no change in the 
    mitigation of an accident will result from this proposed change and 
    no change will occur in the consequences of any accident currently 
    analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        Inadvertent opening of a MSSV is currently analyzed as an 
    initiating event for accidental depressurization of the main steam 
    system. The proposed change does not alter the valves or any other 
    plant component. The valves will continue to perform as analyzed in 
    current accident analyses. The proposed change will not create the 
    possibility for any new or different kind of accident.
        By retaining the use of the HNF trip setpoint reduction, no 
    change is being proposed in the methodology used to ensure that 
    power reductions are carried out; therefore, this will not create 
    the possibility of placing the plant into any new unanalyzed 
    condition. Not adjusting the Nuclear Instrumentation System trip 
    setpoint with the RTBs open will not create an accident. The 
    existing accident analysis is still bounding.
        Combining the separate action statements for 3- and 4-loop 
    operation into a single action does not create the possibility for a 
    new or different kind of accident. Operation with 4 loops will 
    continue to be required in Modes 1 and 2 by TS 3.4.1.1.
        Operation with less than 4 loops will continue to be governed by 
    TS 3.4.1.2 in Mode 3 and TS 3.4.1.3 in Mode 4. This change will not 
    place the plant in a configuration not currently bounded by existing 
    accident analysis.
        Revising the mode requirements and their associated times, 
    consistent with the requirements in NUREG-1431, will continue to 
    ensure that if the unit is unable to comply with the limiting 
    condition for operation, the unit will begin an orderly shutdown 
    until a mode is reached where the specification is not applicable.
        3. Involve a significant reduction in a margin of safety.
        The proposed change reduces the total energy of the reactor 
    coolant system that will ensure the ability of the MSSVs to perform 
    their intended function as assumed in current accident analyses. 
    This change has been evaluated on a generic basis for Westinghouse 
    Electric Corporation designed 4-loop nuclear steam supply systems. 
    SQN plant specific features have been evaluated including power 
    limit calculations and the interaction of the reactor protection 
    system trip time delay and the anticipated transient without scram 
    mitigating system actuation circuitry. Correcting this 
    nonconservatism restores the margin of safety to what was originally 
    envisioned. Therefore, the margin of safety assumed in the accident 
    analysis is not reduced by this change.
        Combining the separate action statements for 3- and 4-loop 
    operation into a single action has no effect on the margin of safety 
    for 4-loop operation with one or more MSSVs inoperable. Under the 
    revised TS, 3-loop operation with one or more MSSVs inoperable would 
    only be allowed in Mode 3, and 4-loop operation will be required in 
    Modes 1 and 2 in accordance with current TSs 3.4.1.1 and 3.4.1.2.
        Revising the mode requirements and their associated times, 
    consistent with the requirements in NUREG-1431, will not reduce the 
    safety margin since the new requirements will continue to place the 
    unit in a mode where the TS is no longer applicable. The new 
    completion times for mode changes are reasonable, based on operating 
    experience, to reach the required unit conditions from full power 
    conditions in an orderly manner without challenging unit systems.
        The margin of safety is unaffected by modifying the limits of 
    Mode 3 applicability to require the RTBs to be closed as the 
    intended safety function is already completed when they are open.
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902.
        NRC Project Director: Frederick J. Hebdon.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: December 9, 1994, and January 27, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Surveillance Requirement 4.6.1.2.a 
    and its associated Bases. The changes would defer the next scheduled 
    containment integrated leak rate test (CILRT) for one outage, from 
    Refuel 7 (March 1995) to Refuel 8 (scheduled for September 1996).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability of 
    occurrence or the consequences of an accident or malfunction of 
    equipment important to safety previously evaluated in the Safety 
    Analysis Report.
        The Callaway CILRT history provides substantial justification 
    for the proposed test schedule. Three CILRTs have been performed 
    over a seven year period with successful results. The tests indicate 
    that Callaway has a low leakage containment. There are no structural 
    mechanisms which would adversely affect the structural capability of 
    the containment and that would be a factor in extending the CILRT 
    schedule by one refueling outage.
        A risk impact assessment was performed, and a determination was 
    made that there is insignificant risk impact as a result of changing 
    the CILRT schedule. Containment leak rate testing is not an 
    initiator of any accident, the proposed interval extension does not 
    affect reactor operations or the accident analysis, and has no 
    radiological consequences. There will be no changes to 10 CFR 100 
    dose limits or the control room dose limits. Extending the test 
    interval will not, by itself, increase the probability of a 
    malfunction of equipment important to safety. Therefore, the 
    proposed change will not involve a significant increase in the 
    probability or consequences of any accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated in the Safety Analysis Report.
        There are no design changes being made that would create a new 
    type of accident or malfunction. The proposed change will not alter 
    the plant or the manner in which it is operated. The change revises 
    the schedule for performing the periodic CILRT. The purpose of the 
    test is to provide periodic verification of the leaktight integrity 
    of the primary reactor containment, and systems and components which 
    penetrate containment. The tests assure that leakage through 
    containment and systems and components penetrating containment will 
    not exceed the allowable leakage rate values associated with 
    [[Page 11142]] conditions resulting from an accident. The change in 
    schedule for performing the CILRT will not adversely affect the 
    containment integrity in the event of an accident. Therefore, the 
    proposed change will not create the possibility of a new or 
    different type of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to the schedule for performing the periodic 
    Type A test does not reduce the margin of safety assumed in the 
    accident analysis for any release of radioactive materials or reduce 
    any margin of safety preserved by the technical specifications. The 
    methodology, acceptance criteria, and the technical specification 
    leakage limits for the performance of the Type A tests will not 
    change. The Type A tests will continue to be performed in accordance 
    with 10 CFR 50, Appendix J and the Callaway Technical 
    Specifications. Therefore, the proposed change will not involve a 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendment request: January 24, 1995.
        Description of amendment request: The proposed amendment would 
    modify Technical Specification (TS) Section 15.6.5, ``Review and 
    Audit,'' and TS Section 15.7.8, ``Administrative Controls.'' The 
    quality assurance audit frequencies would be removed, the section on 
    emergency plan reviews would be removed, and the period for radioactive 
    effluent reporting would be increased to annual. In addition, the 
    references to ``Semiannual Monitoring Report'' would be changed to 
    ``Annual Monitoring Report'' throughout TS Section 15.7.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        In accordance with the requirements of 10 CFR 50.91(a), 
    Wisconsin Electric Power Company (Licensee) has evaluated the 
    proposed changes against the standards of 10 CFR 50.92 and has 
    determined that the operation of Point Beach Nuclear Plant, Units 1 
    and 2, in accordance with the proposed amendments, does not present 
    a significant hazards consideration.
        A proposed facility operating license amendment does not present 
    a significant hazards consideration if operation of the facility in 
    accordance with the proposed amendment will not:
        1. Create a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. Will not create a significant reduction in a margin of 
    safety.
        The proposed changes are administrative in nature. There is no 
    physical change to the facility, its systems, or its operation. 
    Since the changes will allow more flexibility in assigning resources 
    to work on poor or weak performance areas, the plant safety will be 
    enhanced. Operation of PBNP in accordance with the proposed 
    amendments cannot create an increase in the probability or 
    consequences of an accident previously evaluated, create a new or 
    different kind of accident, or result in a significant reduction in 
    a margin of safety. Therefore, the proposed changes do not present a 
    significant hazards consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    To Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Duke Power Company, et al., Docket No. 50-413, Catawba Nuclear Station, 
    Unit 1, York County, South Carolina
    
        Date of amendment request: October 18, 1994.
        Description of amendment request: The proposed amendment would 
    change Technical Specification 3.6.1.2 to defer the next scheduled 
    containment integrated leak rate test at Catawba Unit 1 for one outage, 
    from the end-of-cycle (EOC) 8 refueling outage (scheduled for February 
    1995) to EOC 9 (scheduled for June 1996).
        Date of publication of individual notice in Federal Register: 
    February 6, 1995 (60 FR 7073).
        Expiration date of individual notice: March 8, 1995.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    Duke Power Company, et al., Docket No. 50-413 Catawba Nuclear Station, 
    Unit 1, York County, South Carolina
    
        Date of amendment request: November 29, 1994, as supplemented 
    January 12 and 27, 1995.
        Description of amendment request: The proposed amendment requested 
    renewal for Catawba Unit 1 Cycle 9 operation of the steam generator 
    tube inspection bobbin probe voltage-based interim plugging criteria 
    that had been previously approved for Cycle 8.
        Date of publication of individual notice in Federal Register: 
    February 9, 1995 (60 FR 7801).
        Expiration date of individual notice: March 13, 1995.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    Georgia Power Company, et al., Docket Nos. 50-424 and 50-425, Vogtle 
    Electric Generating Plant, Units 1 and 2, Burke County, Georgia,
    
        Date of amendment request: January 20, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 6.4.1.2 to provide a more accurate 
    description of the Plant Review Board composition.
        Date of publication of individual notice in Federal Register: 
    February 6, 1995 (60 FR 7077). [[Page 11143]] 
        Expiration date of individual notice: March 8, 1995.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia.
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
    
        Date of amendment request: November 7, 1994, as supplemented by 
    letters dated December 20, 1994, and January 23, 1995.
        Brief description of amendment request: The proposed amendments 
    would change the number of diesel generators (emergency power supply) 
    required to be operable during Mode 6 with greater than or equal to 23 
    feet of water above the reactor vessel flange, from two to one. The 
    amendments would also allow limited substitution of an alternate onsite 
    emergency power source for one of the two required diesel generators, 
    in Mode 5 and in Mode 6 with less than 23 feet of water. In addition, 
    changes to certain system specifications that are affected by the 
    changes for the emergency power supply were also proposed.
        Date of individual notice in Federal Register: January 30, 1995 (60 
    FR 5739).
        Expiration date of individual notice: March 1, 1995.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket No. 
    50-461, Clinton Power Station, Unit No. 1, DeWitt County, Illinois
    
        Date of amendment request: January 27, 1995.
        Brief description of amendment request: The amendment modifies the 
    technical specifications (TSs) by eliminating selected response time 
    testing as described in the BWROG topical report NEDO-32291, ``System 
    Analyses for Elimination of Selected Response Time Testing 
    Requirements.'' The affected TSs are TS 3.3.1.1, ``Reactor Protection 
    System (RPS) Instrumentation,'' TS 3.3.5.1, ``Emergency Core Cooling 
    System (ECCS) Instrumentation,'' TS 3.3.6.1, ``Primary Containment and 
    Drywell Isolation Instrumentation,'' and TS 3.5.1, ``ECCS--Operating.''
        Date of publication of individual notice in Federal Register: 
    February 3, 1995 (60 FR 6739).
        Expiration date of individual notice: March 6, 1995.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units 1, 2, 
    and 3, Maricopa County, Arizona
    
        Date of application for amendments: October 31, 1994, as 
    supplemented by letter dated December 28, 1994.
        Brief description of amendments: The amendments revise the 
    refueling machine overload cutoff limit from less than or equal to 1556 
    pounds to less than or equal to 1600 pounds. The change was requested 
    because design and fabrication improvements have increased the weight 
    of the fuel assembly.
        Date of issuance: February 9, 1995.
        Effective date: February 9, 1995, to be implemented within 45 days 
    of the date of issuance.
        Amendment Nos.: 89, 76, and 60.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 6, 1995 (60 FR 
    2160). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units 1, 2, 
    and 3, Maricopa County, Arizona
    
        Date of application for amendments: November 20, 1992, as 
    supplemented by letters dated October 22, 1993, and November 30, 1994.
        Brief description of amendments: The amendments would increase the 
    allowable out-of-service time for the core operating limit supervisory 
    system (COLSS) from 1 hour to 4 hours before the more restrictive 
    limits based on the core protection calculators (CPCs) must be applied.
        Date of issuance: February 14, 1995.
        Effective date: February 14, 1995.
        Amendment Nos.: 90, 77, and 61.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 6, 1993 (58 FR 
    591) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: September 6, 
    1994. [[Page 11144]] 
        Brief description of amendment: The amendment would remove 
    Technical Specification Section 4.5.H.4 which requires the testing and 
    calibration of pressure switches in certain emergency core cooling 
    system lines.
        Date of issuance: February 2, 1995.
        Effective date: February 2, 1995.
        Amendment No.: 157.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 26, 1994 (59 FR 
    53838). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated October 26, 1994 (59 FR 53838).
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of application for amendments: March 25, 1994, as supplemented 
    on July 29, 1994, and August 24, 1994.
        Brief Description of amendments: The amendments change the 
    Technical Specifications to correct several typographical errors, to 
    incorporate material implicitly contained in a footnote to an 
    applicability statement, to provide detailed labels for items listed in 
    a table, to correct the citation of references, and to remove 
    references to the Rod Sequence Control System that should have been 
    included in a previous change.
        Date of issuance: February 1, 1995.
        Effective date: February 1, 1995.
        Amendment Nos.: 174 and 205.
        Facility Operating License Nos. DPR-71 and DPR-62. Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27050). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 1, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
        Date of application for amendment: December 12, 1994.
        Brief description of amendment: The amendment revises the 
    containment spray (CS) nozzle surveillance interval from 5 to 10 years.
        Date of issuance: February 10, 1995.
        Effective date: February 10, 1995.
        Amendment No.: 157.
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    497).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 10, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College, Hartsville, South Carolina 29550.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of application for amendments: June 24, 1994.
        Brief description of amendments: The amendments revise the 
    Technical Specifications by deleting the containment recirculation sump 
    level from Accident Monitoring Instrumentation Tables 3.8.9-1 and 
    4.8.9-1.
        Date of issuance: February 9, 1995.
        Effective date: February 9, 1995.
        Amendment Nos.: 160 and 148.
        Facility Operating License Nos. DPR-39 and DPR-48: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37066).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut, and Northeast Nuclear Energy 
    Company, Docket Nos. 50-245, 50-336, and 50-423, Millstone Nuclear 
    Power Station, Units 1, 2, and 3, New London County, Connecticut
    
        Date of application for amendments: June 30, 1994, as supplemented 
    November 18, 1994, and January 12, 1995.
        Brief description of amendments: The amendments modify the 
    Administrative Controls Section of the Technical Specifications by 
    replacing the present Nuclear Review Board (NRB) for the Haddam Neck 
    Plant, and the NRB and site Nuclear Review Board for Millstone Station 
    with a Nuclear Safety Assessment Board which will serve Millstone Units 
    1, 2, and 3, and Haddam Neck.
        Date of issuance: February 14, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 181, 79, 184, 104.
        Facility Operating License Nos. DPR-61, DPR-21, DPR-65 AND NPF-49.
        Amendments revised the Technical Specifications.
        The November 18, 1994, and January 12, 1995, submittals provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45021).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457, for the Haddam Neck Plant, and Learning 
    Resource Center, Three Rivers Community-Technical College, Thames 
    Valley Campus, 574 New London Turnpike, Norwich, CT 06360, for 
    Millstone 1, 2, and 3.
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley Power 
    Station, Unit No. 1, Shippingport, Pennsylvania
    
        Date of application for amendment: July 29, 1994, as supplemented 
    in a letter dated December 13, 1994.
        Brief description of amendment: This amendment revises Technical 
    Specifications (TSs) 3/4.4.5 and 3.4.6.2 including associated Bases 3/
    4.4.5 and 3/4.4.6.2 to allow the implementation of [[Page 11145]] steam 
    generator tube interim plugging criteria (IPC) for the tube support 
    plate elevations during operating cycle 11. The current TSs require 
    that tubes with imperfections exceeding 40 percent of the nominal tube 
    wall thickness be removed from service. The IPC will allow a test 
    voltage-based criterion of 1.0 volts as determined by a bobbin probe 
    inspection of the tubes. Voltages greater than 1.0 volt will be further 
    examined using a pancake coil probe. Tubes showing flaw indications 
    with a bobbin voltage greater than 3.6 volts will be plugged or 
    repaired.
        Date of issuance: February 3, 1995.
        Effective date: February 3, 1995.
        Amendment No: 184.
        Facility Operating License No. DPR-66. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42337). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 3, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: November 8, 1994.
        Brief description of amendment: The amendment revised the technical 
    specification section that describes the frequency for performing the 
    containment integrated leak rate tests.
        Date of issuance: February 6, 1995.
        Effective date: February 6, 1995.
        Amendment No.: 175.
        Facility Operating License No. DPR-51. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995, (60 FR 
    502). The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 6, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. Lucie 
    Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of application for amendment: July 25, 1994.
        Brief description of amendment: This amendment will upgrade 
    Technical Specification 3/4.7.1.6 for the Main Feedwater Line Isolation 
    Valves to be consistent with NUREG-1432, Standard Technical 
    Specifications for Combustion Engineering Plants.
        Date of Issuance: February 9, 1995.
        Effective Date: February 9, 1995.
        Amendment No.: 71.
        Facility Operating License No. NPF-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45024) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: July 25, 1994.
        Brief description of amendments: These amendments implement GL 93-
    05 Items 5.8, 6.1, 7.1 and 7.5.
        Date of Issuance: February 9, 1995.
        Effective Date: February 9, 1995.
        Amendment Nos.: 133 and 72.
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45023) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas.
    
        Date of amendment request: November 7, 1994.
        Brief description of amendments: The amendments permit both 
    containment personnel airlock doors to be open while moving fuel during 
    refueling operations.
        Date of issuance: February 2, 1995.
        Effective date: February 2, 1995, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 1--Amendment No. 69; Unit 2--Amendment No. 58.
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63123). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
    
        Date of amendment request: November 8, 1994.
        Brief description of amendments: The amendments permit the 
    substitution of an extended range neutron flux monitor for one of the 
    source range neutron flux monitors during refueling operations.
        Date of issuance: February 13, 1995.
        Effective date: February 13, 1995.
        Amendment Nos.: Unit 1--Amendment No. 70; Unit 2--Amendment No. 59.
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63124). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
    
        Date of amendment request: June 6, 1994, as supplemented by letters 
    dated November 17, 1994, and December 5, 1994.
        Brief description of amendments: The amendments modify Technical 
    [[Page 11146]] Specification 3/4.8.1.1, ``A.C. Sources'' by revising 
    the action statements and surveillance requirements for testing of the 
    standby diesel generators (SDGs). The amendments eliminate excessive 
    and unnecessary testing of the SDGs consistent with the guidance 
    provided in NUREG-1366, ``Improvements to Technical Specifications 
    Surveillance Requirements,'' NUREG-1431, ``Standard Technical 
    Specifications for Westinghouse Plants,'' Generic Letter 84-15, 
    ``Proposed Staff Actions to Improve and Maintain Diesel Generator 
    Reliability,'' and Generic Letter 93-05, ``Line-Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operation.'' The changes include: (1) eliminating 
    the requirement to demonstrate the operability of an operable SDG 
    whenever an offsite AC power source is determined to be inoperable, or 
    whenever a support system or an independently testable component of 
    another SDG is inoperable, (2) eliminating the requirement to load the 
    diesel in 10 minutes during testing, (3) replacing the minimum required 
    loading for testing with a load band, (4) relocating some surveillance 
    requirements to the Diesel Fuel Oil Testing Program, and (5) 
    eliminating unnecessary loss-of-offsite power tests.
        Date of issuance: February 2, 1995.
        Effective date: February 2, 1995, to be implemented within 60 days 
    of issuance.
        Amendment Nos.: Unit 1--Amendment No. 68; Unit 2--Amendment No. 57.
        Facility Operating License Nos. NPF-76 and NPF-80. Amendment 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37073). The November 17, 1994, and December 5, 1994, submittals 
    provided clarifying information and did not change the original no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 2, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room Location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
    
        Date of application for amendments: August 3, 1994.
        Brief description of amendments: The amendments relocate the 
    Radiological Effluent Technical Specifications to other controlled 
    documents consistent with NRC Generic Letter 89-01.
        Date of issuance: February 10, 1995.
        Effective date: February 10, 1995.
        Amendment Nos.: 189 and 175.
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55873).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 10, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: October 24, 1994, as 
    supplemented by letter dated December 16, 1994.
        Brief description of amendment: This amendment modifies Technical 
    Specifications Table 4.1-3 surveillance requirements for the new 
    emergency feedwater flow instrumentation. Specifically, the currently 
    installed analog feedwater flow transmitters are to be replaced by new, 
    digital-type flow transmitters. The new digital flow emergency 
    feedwater flow transmitters are continuously self-checking and have a 
    recommended calibration interval of 9 years. The licensee will verify 
    flow whenever the system operates and send one transmitter back to the 
    manufacturer for recalibration every refueling outage.
        Date of issuance: February 15, 1995.
        Effective date: February 15, 1995.
        Amendment No.: 147.
        Facility Operating License No. DPR-36: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63124). The December 16, 1994, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 15, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, Maine 04578.
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: May 25, 1994, as supplemented 
    September 1, 1994, and January 13, 1995.
        Brief description of amendment: This amendment allows (1) entry 
    through an operable personnel air lock hatch to perform surveillance 
    testing, repair an inoperable hatch, or perform other necessary 
    activities inside containment; (2) update plant Technical 
    Specifications to reflect a previous change to the list of containment 
    boundary valves; (3) add a new exception to allow quarterly 
    surveillance testing of the excess flow check valves; (4) add a new 
    exception to allow periodic preventive maintenance on control room 
    ventilation lasting up to 30 minutes per calendar quarter, without a 
    written report of such inoperability; and (5) make related 
    administrative changes to reflect and clarify items 1 through 4 above.
        Date of issuance: February 10, 1995.
        Effective date: February 10, 1995.
        Amendment No.: 146.
        Facility Operating License No. DPR-36: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 22, 1994 (59 FR 
    32231). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 10, 1995.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, Maine 04578.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: November 3, 1993.
        Brief description of amendment: The amendment revises License 
    Condition 2.C.(4), ``Turbine System Maintenance Program,'' and deletes 
    Technical Specification (TS) 3/4.3.8, ``Turbine 
    [[Page 11147]] Overspeed Protection System,'' and its associated Bases. 
    The revision to License Condition 2.C.(4) indicates that the 
    requirements of this license condition have been satisfied. The 
    deletion of TS 3/4.3.8 and its associated Bases provides Niagara Mohawk 
    Power Corporation the flexibility to implement the manufacturer's 
    recommendations for turbine steam valve surveillance test requirements. 
    These test requirements will be contained in the Updated Safety 
    Analysis Report.
        Date of issuance: February 14, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 63.
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64611). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: April 25, 1994.
        Brief description of amendment: The amendment changes the Technical 
    Specifications concerning four related issues: (1) power-operated 
    relief valve and block valve reliability; (2) low-temperature 
    overpressure protection; (3) boron dilution; and (4) shutdown risk 
    management.
        Date of issuance: February 15, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 185.
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27060). The September 21, 1994, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 15, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Thames Valley State Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: June 18, 1993, as supplemented by letter 
    dated November 23, 1994.
        Description of amendment request: The amendment revises the 
    Appendix A Technical Specifications (TS) relating to the Independent 
    Safety Engineering Group. Specifically, the amendment revises the title 
    of TS 6.2.3 from Independent Safety Engineering Group to Independent 
    Technical Reviews, and replaces the requirements for the five person 
    Independent Safety Engineering Group with requirements relating to a 
    technical review program to perform independent technical reviews.
        Date of issuance: February 14, 1995.
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 35.
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 18, 1993 (58 FR 
    43927). The licensee's letter dated November 23, 1994, provided a minor 
    revision to the application but does not change the initial proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 47 
    Front Street, Exeter, NH 03833.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: October 21, 1994.
        Brief description of amendments: These amendments add a test 
    exception to allow reactor coolant temperatures up to 212 degrees F 
    during hydrostatic or inservice leak testing while in OPERATIONAL 
    CONDITION 4 without entering OPERATIONAL CONDITION 3.
        Date of issuance: February 13, 1995.
        Effective date: To be implemented within 30 days from the date of 
    issuance.
        Amendment Nos.: 142 and 112.
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1994 (59 
    FR 66057). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Docket No. 50-353, Limerick Generating 
    Station, Unit 2, Montgomery County, Pennsylvania
    
        Date of application for amendment: December 9, 1993, as 
    supplemented by letters dated July 5, September 9, October 19, November 
    15, and December 2, 1994, January 6 and January 23, 1995. The 
    supplemental letters provided clarifying information that did not 
    change the initial no significant hazards consideration determination.
        Brief description of amendment: This amendment raises the 
    authorized maximum power level from 3293 MWt to a new limit of 3458 
    MWt. The amendment also approves changes to the Technical 
    Specifications to implement uprated power operation.
        Date of issuance: February 16, 1995.
        Effective date: This license amendment is effective as of its date 
    of issuance and is to be implemented prior to startup in Cycle 4.
        Amendment No.: 51.
        Facility Operating License No. NPF-85. This amendment revised the 
    Technical Specifications and License.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7695). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 16, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: October 29, 1993.
        Brief description of amendments: These amendments eliminate the 
    main [[Page 11148]] steamline radiation monitoring system high 
    radiation trip function for initiating (1) an automatic reactor scram 
    and automatic closure of the main steamline isolation valves, and (2) 
    automatic closure of the main steamline drain valves, main steam and 
    reactor water sample line valves. The amendments also approve the 
    relocation of portions of the information contained in the Bases 
    section.
        Date of issuance: February 16, 1995.
        Effective date: February 16, 1995.
        Amendment Nos. 89 and 52.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    624). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 16, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. Ginna 
    Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: May 13, 1994, as supplemented 
    June 24 and September 27, 1994.
        Brief description of amendment: The amendment proposes to amend 
    Appendix A of Operating License DPR-18 to revise Section 6.0 
    ``Administrative Controls'' of the Ginna Technical Specifications (TSs) 
    and would change the title of Senior Vice President, Production and 
    Engineering, include a provision to allow future title changes without 
    license amendment, and implement those changes in NUREG-1431 ``Standard 
    Technical Specification--Westinghouse Plants,'' dated September 1992, 
    by relocating to licensee controlled documents those specifications 
    controlled by regulations and the existing review and audit 
    requirements. The remainder of this amendment request will be reviewed 
    at a later date.
        Date of issuance: February 6, 1995.
        Effective date: February 6, 1995.
        Amendment No.: 58.
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37084). The June 24, 1994, submittal provided information which did not 
    change the initial no significant hazards consideration determination. 
    The licensee's submittal of September 27, 1994, limited, but did not 
    change, the licensee's previously requested TS changes of May 13, 1994.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 6, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of application for amendments: December 30, 1993, as 
    supplemented by letters dated June 3, 1994, August 25, 1994, and 
    January 3, 19, and 30, 1995.
        Brief description of amendments: These amendments will revise TS 
    Table 3.3-1, ``Reactor Protective Instrumentation,'' to allow the use 
    of the source range neutron flux monitors in place of safety related 
    excore monitors in Modes 3, 4, and 5, with the reactor trip circuit 
    breakers open or the Control Element Assembly (CEA) Drive System not 
    capable of CEA withdrawal, for the purpose of monitoring core reactive 
    changes.
        Date of issuance: February 13, 1995.
        Effective date: February 13, 1995.
        Amendment Nos.: 115 and 104.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49434). The additional information contained in the January 3, 19, 
    and 30, 1995, letters were clarifying in nature, within the scope of 
    the initial notice and did not affect the NRC staff's proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of application for amendments: July 28, 1994, as supplemented 
    by letters dated January 30 and February 13, 1995.
        Brief description of amendments: These amendments propose to revise 
    Technical Specification (TS) 3.9.8.1 ``Shutdown Cooling and Coolant 
    Circulation--High Water Level,'' TS 3.9.8.2 ``Shutdown Cooling and 
    Coolant Circulation--Low Water Level,'' and their Bases to facilitate 
    testing of low-pressure safety injection system components and permit 
    additional flexibility in scheduling maintenance on the shutdown 
    cooling system.
        Date of issuance: February 15, 1995.
        Effective date: February 15, 1995.
        Amendment Nos.: 116 and 105.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications on a one-time basis for each unit.
        Date of initial notice in Federal Register: October 12, 1994 (59 FR 
    51627). The additional information contained in the supplemental 
    letters dated January 30 and February 13, 1995, served to clarify the 
    amendments, was within the scope of the initial notice, and did not 
    affect the Commission's proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 15, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    South Carolina Electric & Gas Company, South Carolina Public Service 
    Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit 
    No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: October 17, 1994, as 
    supplemented January 30, 1995.
        Brief description of amendment: The amendment changes the Technical 
    Specifications to relocate the seismic monitoring instrumentation (SMI) 
    Limiting Condition for Operation (LCO), Surveillance Requirements 
    (SRs), and associated tables and bases contained in Technical 
    Specifications (TS) sections 3.3.3.3 and 4.3.3.3 to the Final Safety 
    Analysis Report (FSAR) or an equivalent controlled document.
        Date of issuance: February 15, 1995.
        Effective date: February 15, 1995.
        Amendment No.: 122.
        Facility Operating License No. NPF-12. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 8, 1994 (59 FR 
    55717). The January 30, 1995, supplement did not affect the staff's 
    [[Page 11149]] finding of no significant hazards consideration.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 15, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: September 29, 1993.
        Brief Description of amendment: The proposed changes revise 
    standards for testing of charcoal used for removal of radioactive 
    iodine in ventilation systems at the Browns Ferry Nuclear Plant.
        Date of issuance: February 13, 1995.
        Effective Date: February 13, 1995.
        Amendment Nos.: 215, 231 and 188.
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67862). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 13, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room Location: Athens Public library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket No. 50-296, Browns Ferry Nuclear 
    Plant, Unit 3, Limestone County, Alabama
    
        Date of application for amendment: March 29, 1994.
        Brief Description of amendment: The amendment adds requirements for 
    load shedding components being added to ensure that emergency diesel 
    generators are not overloaded during design basis accidents.
        Date of issuance: February 14, 1995.
        Effective Date: February 14, 1995.
        Amendment No.: 189.
        Facility Operating License No. DPR-68: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39597). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 14, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room Location: Athens Public library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: December 16, 1994; supplemented 
    January 19, 1995 (TS 94-16).
        Brief description of amendments: The amendments remove the 900 rpm 
    emergency diesel generator surveillance test criteria and a requirement 
    that the plant be shutdown for performance of the interdependence 
    diesel generator tests.
        Date of issuance: February 9, 1995.
        Effective date: February 9, 1995.
        Amendment Nos.: 195 and 186.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: December 29, 1994 (59 
    FR 67350). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 9, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has [[Page 11150]] made a determination based on 
    that assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By March 31, 1995, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    Commonwealth Edison Company, Docket No. 50-374, LaSalle County Station, 
    Unit 2, LaSalle County, Illinois
    
        Date of application for amendment: January 30, 1995.
        Brief description of amendment: The amendment adds a footnote to 
    Technical Specification Table 4.3.1.1-1 to allow a one-time extension 
    of the surveillance interval for the main steam line isolation valve 
    (MSIV) closure reactor protection system channel functional test. This 
    extension averts the need to perform the functional test prior to the 
    start of the upcoming Unit 2 refueling outage.
        Date of Issuance: February 15, 1995.
        Effective date: Immediately and shall be implemented prior to 2:45 
    a.m. CST on February 15, 1995.
        Amendment No.: 86.
        Facility Operating License No. NPF-18: The amendment revised the 
    Technical Specifications.
        Press release issued requesting comments as to proposed no 
    siginificant hazards consideration: Yes. February 6, 1995, Morris Daily 
    Herald; Ottawa Daily Times; and Streator Times-Press.
        Comments received: No. The Commission's related evaluation of the 
    amendment, finding of exigent circumstances, consultation with the 
    State of Illinois and final determination of no significant hazards 
    consideration [[Page 11151]] are contained in a Safety Evaluation dated 
    February 14, 1995.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348.
        NRC Project Director: Robert A. Capra.
    
        Dated at Rockville, Maryland, this 21st day of February 1995.
    
        For the Nuclear Regulatory Commission.
    John N. Hannon,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 95-4870 Filed 2-28-95; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Published:
03/01/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-4870
Dates:
February 9, 1995, to be implemented within 45 days of the date of issuance.
Pages:
11125-11151 (27 pages)
PDF File:
95-4870.pdf