X96-10313. Biweekly Notice  

  • [Federal Register Volume 61, Number 50 (Wednesday, March 13, 1996)]
    [Notices]
    [Pages 10391-10406]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-10313]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from February 16, 1996, through March 1, 1996. 
    The last biweekly notice was published on February 28, 1996 (61 FR 
    7542).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By April 12, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one
    
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    contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: September 16, 1994, as supplemented on 
    January 31, 1996.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications to eliminate periodic response time 
    testing requirements for selected pressure and differential pressure 
    sensors in the reactor trip system and engineered safety features 
    actuation instrumentation channels.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 50.91(a), the licensee has provided 
    its analysis of the issue of no significant hazards consideration, 
    which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This change to the Technical Specifications does not result in a 
    condition where the design, material, and construction standards 
    that were applicable prior to the change are altered. The same RTS 
    and ESFAS instrumentation is being used; the time response 
    allocations/modeling assumptions in the Updated Final Safety 
    Analysis Report (UFSAR), Chapter 15, Accident Analyses, are still 
    the same; only the method of verifying time response is changed. The 
    proposed change will not modify any system interface and could not 
    increase the likelihood of an accident since these events are 
    independent of this change. The proposed activity will not change, 
    degrade or prevent actions or alter any assumptions previously made 
    in evaluating the radiological consequences of an accident described 
    in the UFSAR. Therefore, the proposed amendment does not result in 
    any increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This change does not alter the performance of the identified 
    pressure and differential pressure transmitters and switches used in 
    the plant protection systems. All sensors will still have response 
    time verified by test before placing the sensor in operational 
    service, and after any maintenance that could affect response time. 
    Changing the method of periodically verifying instrument response 
    for these sensors (assuring equipment operability) from time 
    response testing to calibration and channel checks does not result 
    in any design, installation, or operational changes and thus will 
    not create any new accident initiators or scenarios. Periodic 
    surveillance of these instruments will detect significant 
    degradation in the sensor response characteristics. Implementation 
    of the proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        This change does not affect the total system response time 
    assumed in the safety analyses. The periodic system response time 
    verification method for the identified pressure and differential 
    pressure sensors and switches is modified to allow use of (1) 
    historical records based on acceptable response time tests 
    (hydraulic, noise, or power interrupt tests), (2) inplace, onsite or 
    offsite (e.g. vendor) test measurements, or (3) using vendor 
    engineering specifications.
        The method of verification still provides assurance that the 
    total system response is within that defined in the safety analyses, 
    since calibration tests will detect any degradation which might 
    significantly affect sensor response time. Based on the above, it is 
    concluded that the proposed license amendment request does not 
    result in a reduction in margin with respect to plant safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley 
    Power Station, Unit No. 1, Shippingport, Pennsylvania
    
        Date of amendment request: February 12, 1996
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 4.6.2.2.d to delete the reference 
    to the specific test acceptance criteria for the Containment 
    Recirculation Spray Pumps and replace the specific test acceptance 
    criteria with
    
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    reference to the requirements of the Inservice Testing (IST) Program. 
    In addition, the 18-month test frequency would be replaced with the 
    test frequency requirements specified in the IST Program. The proposed 
    amendment would make this TS the same as Beaver Valley Power Station, 
    Unit No. 2 TS 4.6.2.2.d which was revised by License Amendment No. 68 
    on May 3, 1995.
        The proposed amendment would also revise the Bases of TS 4.6.2.2.d 
    for both Unit Nos. 1 and 2 to describe the proposed revision to TS 
    4.6.2.2.d.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 50.91(a), the licensee has provided 
    its analysis of the issue of no significant hazards consideration, 
    which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The change does not result in a modification to plant equipment 
    nor does if affect the manner in which the plant is operated. The 
    Recirculation Spray System (RSS) pumps are normally in a standby 
    condition and only operate during accident mitigation. Since the 
    physical plant equipment and operating practices are not changed, as 
    noted above, there is no change in the probability of an accident 
    previously evaluated.
        The proposed change, for Beaver Valley Power Station (BVPS) Unit 
    No. 1 only, will not lower the pump performance operability criteria 
    for the RSS pumps. The required values for developed pump head and 
    flow will continue to satisfy accident mitigation requirements and 
    will be maintained and controlled in the BVPS Unit No. 1 Inservice 
    Testing (IST) Program.
        Since the proposed change does not lower the RSS pump 
    performance acceptance criteria, the containment depressurization 
    system will continue to meet its design basis requirements. The 
    proposed change will not impose additional challenges to the 
    containment structure in terms of peak pressure. The calculated 
    offsite does consequences of a design basis accident (DBA) will 
    remain unchanged since the one hour release duration remains 
    unchanged. Future changes to the RSS pump head and flow requirements 
    will be made under the 10 CFR 50.59 process to ensure that the 
    containment performance requirements continue to be met.
        The proposed change in the RSS pump surveillance interval from 
    18 months to every refueling, will not affect the ability of the 
    pumps to perform as assumed in the Safety Analyses. The proposed 
    change to the Bases section, for BVPS Unit Nos. 1 and 2, will ensure 
    that safety analyses assumptions for assumed pump performance 
    continue to be met. The words ``required developed head'' will be 
    clearly defined to reflect that they refer to the value assumed in 
    the safety analysis for the recirculation spray pump's developed 
    head at a specific point. The proposed changes to the Index pages 
    are administrative in nature and do not affect plant safety. 
    Therefore, the proposed change does not involve a significant 
    increase in the consequences of an accident previously evaluated.
        Based on the above discussion, it is concluded that this change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not alter the method of operating the 
    plant. The recirculation spray system is an accident mitigation 
    system and is normally in standby. System operation would be 
    initiated following a containment pressure increase resulting from a 
    DBA. The RSS pumps will continue to provide sufficient flow to 
    mitigate the consequences of a DBA. RSS operation continues to 
    fulfill the safety function for which it was designed and no changes 
    to plant equipment will occur. As a result, an accident which is new 
    or different than any already evaluated in the Updated Final Safety 
    Analysis Report will not be created due to this change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The surveillance requirements for demonstrating that the RSS 
    pumps are operable will continue to assure the ability of the system 
    to satisfy its design function. Therefore, the proposed change will 
    not affect the ability of the RSS to perform its safety function.
        The containment spray system design requirement to restore the 
    containment to subatmospheric condition within one hour will 
    continue to be satisfied. This proposed change does not have any 
    affect on the containment peak pressure since the containment peak 
    pressure occurs prior to the initiation of any of the two 
    containment spray systems. There is no resultant change in dose 
    consequences since the containment will continue to reach a 
    subatmospheric pressure within the first hour following a DBA.
        The RSS pumps' performance requirements will continue to be 
    controlled in a manner to ensure safety analysis assumptions are 
    met.
        Therefore, based on the above discussion, it can be concluded 
    that the proposed change does not involve a significant reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of amendment request: November 30, 1995
        Description of amendment request: The proposed amendment would 
    implement the Option I-D long-term stability solution and remove the 
    existing SIL-380 Rev. 1-based specifications. In addition, the proposed 
    change would require a plant scram be initiated should the plant enter 
    natural circulation conditions and would prohibit restarting a 
    recirculation pump while in natural circulation. The proposed change 
    would define natural circulation. Finally, this change would delete 
    Technical Specification (TS) actions and surveillance requirements 
    related to core plate differential pressure noise while in single 
    recirculation pump operation (SLO).
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        1) The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The implementation of the [boiling water 
    reactor] BWR Owner's Group long term solution Option I-D does not 
    modify the assumptions in the existing accident analysis. The use of 
    an exclusion region and the operator actions required to avoid and 
    minimize operation inside the region do not increase the possibility 
    of an accident. Licensing Topical Report, 'Evaluation of the 
    ``Regional Exclusion with Flow-Biased APRM [average power range 
    monitor] Neutron Flux Scram'' Stability Solution', GENE-A000-04021-
    01 (attachment 1) demonstrates that the APRM flow-biased scram 
    function provides a high degree of assurance that the fuel safety 
    limit will not be exceeded should power oscillations occur during 
    plant operation within the restricted region. Regional mode core 
    oscillations are not predicted to occur at the [Duane Arnold Energy 
    Center] DAEC because of its small core size and tight core inlet 
    orifices. Conditions for operation outside of the exclusion region 
    are within the assumptions of the existing accident analysis. The 
    operator action requirement to exit the exclusion region upon entry 
    minimizes the probability of an instability event occurring. 
    Inserting control rods or increasing recirculation flow, the 
    evolutions to be used to exit the region, are normal plant 
    maneuvers.
        The proposed clarifications to explicitly direct the operator to 
    initiate a reactor scram
    
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    in the event of operation in natural circulation are conservative 
    and consistent with current plant operating practices. Likewise, the 
    proposed prohibition from starting a recirculation pump as a means 
    of exiting the natural circulation mode of operation is also 
    conservative. Therefore, the proposed license amendment does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The core plate differential pressure noise surveillances that 
    are performed while in single recirculation pump operation were 
    included in TS Amendment 119 due to NRC concerns at the 
    time that high core plate noise observed during [single-loop 
    operation] SLO at Brown's Ferry in 1985 could be an indication of 
    thermal hydraulic instability. [General Electric] GE has since 
    determined that core plate differential pressure noise is not a 
    cause of thermal hydraulic instability and that the noise does not 
    pose a safety concern. Therefore, the proposed license amendment 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2) The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated. As stated above, the proposed changes either 
    mandate operation within the envelope of previously analyzed plant 
    operating conditions or direct the operator to immediately return 
    the plant to within these analyzed conditions using normal plant 
    maneuvers. In addition, analysis has demonstrated that the APRM 
    flow-biased scram function provides a high degree of assurance that 
    the fuel safety limit will not be exceeded should power oscillations 
    occur during plant operation within the restricted region. 
    Therefore, the potential for a new or different type of accident 
    from those previously evaluated is not created.
        The proposed clarifications to explicitly direct the operator to 
    initiate a reactor scram in the event of operation in natural 
    circulation are conservative and consistent with current plant 
    operating practices. Likewise, the proposed prohibition from 
    starting a recirculation pump as a means of exiting the natural 
    circulation mode of operation is also conservative. Therefore, the 
    potential for a new or different type of accident from those 
    previously evaluated is not created.
        The core plate differential pressure noise surveillances that 
    are performed while in single recirculation pump operation were 
    included in TS Amendment 119 due to NRC concerns at the 
    time that high core plate noise observed during SLO at Brown's Ferry 
    in 1985 could be an indication of thermal hydraulic instability. GE 
    has since determined that core plate differential pressure noise is 
    not a cause of thermal hydraulic instability and that the noise does 
    not pose a safety concern. Therefore, the potential for a new or 
    different type of accident from those previously evaluated is not 
    created.
        3) The proposed amendment will not reduce the margin of safety. 
    The combination of the proposed requirements to avoid possible 
    unstable conditions and the automatic flow biased high reactor flux 
    scram provide defense in depth to provide fuel protection. Therefore 
    the individual or combination of means to detect and suppress 
    thermal hydraulic instability supplements the margin of safety.
        The proposed specification related to initiating a reactor scram 
    while in natural circulation is conservative. Likewise, the proposed 
    prohibition from starting a recirculation pump as a means of exiting 
    the natural circulation mode of operation is also conservative and 
    therefore does not constitute a reduction in the margin of safety.
        The core plate differential pressure noise surveillances that 
    are performed while in single recirculation pump operation were 
    included in TS Amendment 119 due to NRC concerns at the 
    time that high core plate noise observed during SLO at Brown's Ferry 
    in 1985 could be an indication of thermal hydraulic instability. GE 
    has since determined that core plate differential pressure noise is 
    not a cause of thermal hydraulic instability and that the noise does 
    not pose a safety concern. Therefore, the elimination of these 
    surveillance tests does not constitute a reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401
        Attorney for licensee: Jack Newman, Kathleen H. Shea, Morgan, 
    Lewis, & Bockius, 1800 M Street, NW., Washington, DC 20036-5869
        NRC Project Director: Gail H. Marcus
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: November 16, 1995
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to add a Limiting Condition 
    for Operation and surveillance test for safety related inverters and 
    deletes requirements for non-safety related instrument buses.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes will delete requirements from the Technical 
    Specifications (TS) for non-safety related 120 Volt a-c instrument 
    panels AI-42A and AI-42B, and incorporate new requirements for the 
    safety-related 125 Volt d-c to 120 Volt a-c inverters (A, B, C, and 
    D) similar to the Standard Technical Specification for Combustion 
    Engineering plants as contained in NUREG-1432.
        TS 2.7 requires that 120 Volt instrument panels AI-42A and AI-
    42B be operable whenever the reactor coolant temperature is above 
    300 F. Either of these instrument panels may be inoperable for up 
    to 8 hours or a plant shutdown is required. These instrument panels 
    are non-safety related and do not receive or actuate any Engineered 
    Safeguards Features (ESF) or Reactor Protection System (RPS) and the 
    panels are not required for, nor do they indicate the status of, 
    containment integrity. The FCS plant specific Probabilistic Risk 
    Assessment (PRA) model was reviewed to determine the effect of 
    unavailability of these instrument panels on the core damage 
    frequency. The results of the review show that the unavailability of 
    these panels is not a contributor to risk. Therefore these 
    instrument panels do not meet any of the four criteria contained in 
    10 CFR 50.36 for inclusion into TS. The operation of these panels 
    are controlled by plant procedures that are governed by 10 CFR 
    50.59.
        Therefore, deletion of the requirements for AI-42A and AI-42B 
    from the TS would not significantly increase the probability or 
    consequences of an accident previously evaluated.
        It is also proposed to incorporate new requirements for the 
    safety-related 125 Volt d-c to 120 Volt a-c inverters (A, B, C, and 
    D). Currently, there are no TS requirements for inoperability of the 
    safety-related inverters. However, if an inverter is inoperable and 
    its associated 120 Volt a-c instrument bus is powered by its safety-
    related bypass transformer, the a-c instrument bus is considered 
    inoperable and an 8 hour Limiting Condition for Operation is 
    applied. The bus is declared inoperable even though it is being 
    powered from a safety related power source because this source is 
    not an uninterruptible power supply. Operating experience has shown 
    that, in many instances, 8 hours is insufficient time to 
    troubleshoot and conduct repairs on an inverter. FCS initiated a TS 
    required plant shutdown in November 1994, and again in January 1995, 
    due to inoperable inverters that could not be repaired in the 8 
    hours allowed by TS. If FCS had 24 hours to conduct repairs, a power 
    reduction, and the potential to challenge plant systems, would not 
    have been necessary.
        The proposed change does not increase the probability of an 
    accident since loss of power to a vital bus is not an initiator of 
    any analyzed accident. The proposed change does not increase the 
    consequences of any accident since the TS currently allow one 120 V 
    instrument bus to be inoperable and de-energized. The proposed 
    change would only allow one 120 V instrument bus to be energized 
    from a safety related bypass source. The proposed changes do not 
    reduce the number of RPS or ESF actuation channels that are required 
    to be operable. Should a
    
    [[Page 10396]]
    loss of offsite power event occur, power to the instrument bus would 
    only be interrupted during the time required for the emergency 
    diesel generator to start and load.
        The FCS plant specific PRA model was reviewed to determine the 
    effect of unavailability of the 120 V instrument panels supplied by 
    inserters A, B, C, and D on the core damage frequency. The results 
    of the review show that the loss of one of the panels has an 
    insignificant effect on the PRA model. Therefore, the proposed 
    change of allowing a 24 hour period with one instrument panel 
    powered from a interruptible power supply has a insignificant effect 
    on the PRA results.
        Therefore, the proposed change to include specific operability 
    requirements for safety related inverters does not significantly 
    increase the probability or consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There will be no physical alterations to the plant 
    configuration, changes to setpoint values, or changes to the 
    implementation of setpoints or limits as a result of these proposed 
    changes. The proposed changes do not reduce the number of RPS or ESF 
    actuation channels that are required to be operable. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes delete TS requirements for nonsafety 
    related instrument panels and incorporate additional operability 
    requirements for safety related inverters. The proposed changes do 
    not revise any setpoints or limits monitored by the instrument 
    panels or buses. In addition, a review of the FCS plant specific PRA 
    shows that these proposed changes are insignificant to core damage 
    frequency. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William H. Bateman
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
        Date of amendment request: February 1, 1996
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) to allow an increase in the 
    initial nominal enrichment limit of fuel assemblies to be stored in the 
    spent fuel pool.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change to the Technical Specifications to increase 
    the enrichment limit for fuel assembly storage requirements does not 
    involve a significant increase in the probability of an accident. 
    The enrichment limit is not a precursor to any analyzed event and 
    therefore cannot impact probability.
        The safety evaluation for the existing Spent Fuel Pool (SFP) 
    storage racks was approved by the NRC in Amendment 155 (TAC M85116). 
    This amendment approved the current limit on fuel enrichment, and 
    the mechanical, structural, and thermal/hydraulic design of the fuel 
    racks. This amendment also evaluated the radiological consequences 
    of a fuel handling accident with fuel enrichments equivalent to the 
    proposed change. The proposed change will not impact this previously 
    approved evaluation with the exception of the nuclear criticality 
    analysis. The nuclear criticality analysis supporting the proposed 
    change used calculational methods conforming to NRC guidance, 
    industry codes, standards, and specifications. In meeting the 
    acceptance criteria for criticality in the SFP, such that keff 
    is always less than or equal to O.95 at a 95%/95% probability 
    tolerance level, the proposed change from 4.2 weight percent (w/o) 
    to 4.5 w/o Uranium-235 (U235) does not involve an increase in 
    the consequences of an accident previously evaluated.
        Therefore, it is concluded that the proposed change to increase 
    the enrichment limit for fuel storage does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change was evaluated in accordance with the 
    guidance of the NRC Position Paper entitled, ``OT Position for 
    Review and Acceptance of Spent Fuel Storage and Handling 
    Applications'', appropriate sections of the NRC Standard Review 
    Plan, Regulatory Guides, industry codes, and standards. In addition, 
    the NRC Safety Evaluation Report for Amendment 155 was also reviewed 
    with respect to the proposed change.
        No new or different mode of operation is proposed. No unproven 
    technology was utilized in the analytical techniques necessary to 
    justify the planned fuel storage change. The analytical techniques 
    used have been developed and used in over 15 applications previously 
    approved by the NRC. Based upon the reviews, it is concluded that 
    the proposed change does not create the possibility of a new or 
    different type accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The only margin of safety potentially impacted by the proposed 
    change is related to nuclear criticality considerations. The 
    established acceptance criterion for criticality is that the neutron 
    multiplication factor in spent fuel pools shall be less than or 
    equal to 0.95, including all uncertainties, under all conditions. 
    This margin of safety has been adhered to in the criticality 
    analysis methods for the proposed change. Therefore the proposed 
    change does not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William H. Bateman
    PECO Energy Co., Public Service Electric and Gas Co., Delmarva 
    Power and Light Co., and Atlantic City Electric Co., Dockets Nos. 
    50-277 and 50-278, Peach Bottom Atomic Power Station, Units Nos. 2 
    and 3, York County, Pennsylvania
        Date of application for amendments: December 21, 1995
        Description of amendment request: The proposed amendments would 
    modify the Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3 
    Facility Operating Licenses (FOLs) to provide for elimination of 
    outdated or superseded material regarding, among other things, 
    environmental monitoring and modifications to the low pressure coolant 
    injection system, and for making the FOL of Unit 2 consistent with the 
    FOL of Unit 3.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        The changes proposed in the Application do not constitute a 
    Significant Hazards Consideration in that:
        i) The proposed changes do not involve a significant increase in 
    the probability or
    
    [[Page 10397]]
    
    consequences of an accident previously evaluated because the changes 
    are purely administrative and do not involve any physical changes to 
    plant SSC [structures, systems, and components]. Therefore, these 
    changes will not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        ii) The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because the changes will not alter the plant or the manner in which 
    the plant is operated. The changes do not allow plant operation in 
    any mode that is not already evaluated in the safety analysis. The 
    changes will not alter assumptions made in the safety analysis and 
    licensing bases. Therefore, these changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        iii) The proposed changes do not involve a significant reduction 
    in a margin of safety because they are purely administrative and 
    have no impact on any safety analysis assumptions.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    Pennsylvania 19101
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket No. 50-388, 
    Susquehanna Steam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: January 11, 1996
        Description of amendment request: The proposed amendment adds a new 
    action statement to Section 3.8.3.1. of the Technical Specifications 
    which precludes the need for entry into Limiting Condition for 
    Operation (LCO) 3.0.3 to allow the performance of certain Emergency 
    Diesel Generator testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 50.91(a), the licensee has provided 
    its analysis of the issue of no significant hazards consideration, 
    which is presented below:
        The proposed changes do not:
        I. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to allow 8 hours to perform Emergency Diesel 
    Generator testing and eliminate the need to enter LCO 3.0.3 to 
    perform this testing does not increase the chances for a previously 
    analyzed accident to occur. The 8 hour time limit before requiring a 
    unit shutdown balances the benefit of performing the required test 
    with the low probability of a LOCA/LOOP [loss-of-coolant accident/
    loss of offsite power] while being in the degraded condition for the 
    duration of the test. To ensure that this risk is minimized, a 
    significant amount of precautions are taken prior to test 
    initiation. The governing surveillance procedures have a very 
    restrictive list of test prerequisites and limitations, which ensure 
    the availability of remaining ac [alternating current] electrical 
    power distribution systems and reduce the potential for any single 
    failure. The allowance of 8 hours to complete the required test 
    prior to initiating shutdown actions ensures operator attention is 
    focused on minimizing the potential loss of power to the remaining 
    division, and restoring power to the effected division upon test 
    completion; thus, not redirecting operator attention towards a plant 
    shutdown per 3.0.3. Therefore, the proposed change will not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        II. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Inhibiting the ESS [electronic switching system] Buses in Unit 1 
    requires that an LCO be entered in Unit 2 due to the common loads 
    shared between the Units. However, performance of the LOCA/LOOP or 
    LOOP surveillance procedures does not cause any diesel generator to 
    become inoperable as a result of inhibiting an ESS Bus. The time 
    frame the diesels are fully loaded in the testing evolution is for a 
    five-minute period to fulfill a Technical Specification requirement. 
    If at that precise moment a LOCA/LOOP occurs in the operating unit, 
    the ESS Buses in Unit 1 and 2 will de-energize except for the ESS 
    Buses that are already connected to the diesels. In the first few 
    minutes of a postulated LOCA/LOOP occurring in the operating Unit 
    while performing a LOCA/LOOP test, the operator would have to take 
    immediate action to shed non-essential loads from the diesels in the 
    Unit under test to prepare the diesels for the shutdown loads via 
    the load sequence timers in the operating unit. Existing emergency 
    procedures require that these actions will be taken. Therefore, the 
    incorporation of this change will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        III. Involve a significant reduction in a margin of safety.
        With one or more required ac buses, (two load groups) de-
    energized, the remaining ac electrical power distribution subsystems 
    are capable of supporting the minimum safety functions necessary to 
    shutdown the reactor and maintain it in a safe shutdown condition, 
    assuming no single failure. The overall reliability is reduced, 
    however, because a single failure in the remaining power 
    distribution subsystems could result in the minimum required ESF 
    [engineered safety feature] functions not being supported. 
    Therefore, the required ac buses must be restored to OPERABLE status 
    within a relatively short period of time. Eight hours has been 
    accepted by the NRC as documented in NUREG-1433, Revision 1, 
    ``Standard Technical Specifications.'' Therefore, the incorporation 
    of this change will not involve a significant reduction in the 
    margin to safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) 
    aresatisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: February 5, 1996
        Description of amendment request: The proposed amendment would 
    revise Davis-Besse Nuclear Power Station (DBNPS) Technical 
    Specification (TS) 3/4.3.2.1 - Safety Features Actuation System 
    Instrumentation and its associated Bases. The revision changes the 
    following items in the Sequence Logic Channels portion of Table 3.3-3: 
    Functional Unit 4.a, Sequencer; Functional Unit 4.b, Essential Bus 
    Feeder Breaker Trip (90%); Functional Unit 4.c, Diesel Generator Start, 
    Load Shed on Essential Bus (59%); and the associated Bases, to clarify 
    the design and actuation logic and to specify actions to take if 
    instrumentation channels become inoperable.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        Toledo Edison has reviewed the proposed changes and determined 
    that a significant hazards consideration does not exist because 
    operation of the Davis-Besse Nuclear Power Station, Unit No. 1 in 
    accordance with these changes would:
        1a. Not involve a significant increase in the probability of an 
    accident previously
    
    [[Page 10398]]
    evaluated because the proposed change to accurately reflect the 
    design and actuation logic of the sequencers and essential bus 
    undervoltage relays, and provide TS actions for two inoperable 
    functional units does not make a change to any accident initiator, 
    initiating condition or assumption. The accident previously 
    evaluated in the DBNPS Updated Safety Analysis Report (USAR) Section 
    15.2.9, Loss of All AC Power to the Station Auxiliaries (Station 
    Blackout), is not affected by this proposed change. The proposed 
    action statements maintain the USAR requirement for starting and 
    loading of one [emergency diesel generator] EDG to meet the minimum 
    [engineered safety features] ESF requirements. The proposed change 
    accurately reflects the plant design, therefore, the change does not 
    involve a significant change to the plant design or operation.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because the proposed changes do not 
    invalidate assumptions used in evaluating the radiological 
    consequences of an accident, do not alter the source term or 
    containment isolation and do not provide a new radiation release 
    path or alter potential radiological releases.
        2. Not create the possibility of a new or different kind of 
    accident from any accident previously evaluated because the proposed 
    changes do not introduce a new or different accident initiator or 
    introduce a new or different equipment failure mode or mechanism.
        3. Not involve a significant reduction in a margin of safety 
    because the proposed changes do not reduce the margin to safety 
    which exists in the present TS or USAR. The proposed changes permit 
    continued operation with one unit of the sequencer, 59% or 90% 
    undervoltage protection inoperable provided the unit is placed in 
    the tripped condition which is consistent with the current TS. With 
    two units of the same function inoperable the associated EDG is 
    declared inoperable and the requirements of the TS for an inoperable 
    EDG entered, including verification that the requirements of TS 
    3.0.5 are met to assure that the minimum ESF requirement is met. The 
    operability requirements of the proposed TS are consistent with the 
    initial condition assumptions of the safety analyses.
        The NRC staff has reviewed the licensees' analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: February 5, 1996
        Description of amendment request: The proposed amendment would 
    correct typographical errors, textual inconsistencies, and minor 
    errors. In addition, equipment identification numbers would be added to 
    the tables.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        1. The administrative changes proposed herein will have no 
    effect on plant hardware, plant design, safety limit setting, or 
    plant system operation and therefore do not modify or add any 
    initiating parameters that would significantly increase the 
    probability or consequences of any previously analyzed accident.
        2. These changes do not affect any equipment nor do they involve 
    any potential initiating events that would create any new or 
    different kind of accident. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. These changes do not affect any equipment involved in 
    potential initiating events or safety limits. Therefore, it is 
    concluded that the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301
        Attorney for licensee: R. K. Gad, III, Ropes and Gray, One 
    International Place, Boston, MA 02110-2624
        NRC Project Director: Ledyard B. Marsh
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: February 8, 1996
        Description of amendment request: The proposed amendments will 
    modify Technical Specification Section 15.3.10, ``Control Rod and Power 
    Distribution Limits,'' and Section 15.4.1, ``Operational Safety 
    Review.'' Changes and additions are proposed to clarify the 
    specifications and to more closely conform to current staff guidance.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration which is presented 
    below:
        1. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The probabilities of accidents previously evaluated are based on 
    the probability of initiating events for these accidents. Initiating 
    events for accidents previously evaluated for Point Beach include: 
    control rod withdrawal and drop, CVCS [chemical and volume control 
    system] malfunction (boron dilution), startup of an inactive reactor 
    coolant loop, reduction in feedwater enthalpy, excessive load 
    increase, losses of reactor coolant flow, loss of external 
    electrical load, loss of normal feedwater, loss of all AC power to 
    the auxiliaries, turbine overspeed, fuel handling accidents, 
    accidental releases of waste liquid or gas, steam generator tube 
    rupture, steam pipe rupture, control rod ejection, and primary 
    coolant system ruptures.
        The consequences of the accidents previously evaluated in the 
    PBNP [Point Beach Nuclear Plant] FSAR [Final Safety Analysis Report] 
    are determined by the results of analyses that are based on initial 
    conditions of the plant, the type of accident, transient response of 
    the plant, and the operation and failure of equipment and systems.
        This change request proposes to improve the clarity of the 
    requirements concerning shutdown margin, rod group alignment limits, 
    rod position indication, bank insertion limits, power distribution 
    limits, at-power physics tests exceptions, and low power physics 
    tests exceptions. The proposed changes do not affect the probability 
    of any accident initiating event, because these Technical 
    Specification requirements do not control any factors that could be 
    accident initiators. These Technical Specifications establish the 
    requirements that provide the limitations on the initial conditions, 
    transient response of the plant, and operation and failure of 
    equipment and systems. The proposed changes establish the 
    appropriate limiting conditions for operation, action statements, 
    and allowable outage times that will continue to ensure that the 
    results of the accident analyses are not changed. Additionally, 
    there is no physical change to the facility or its systems. 
    Therefore, the probability and consequences of any accident 
    previously evaluated is not increased.
        2. Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        New or different kinds of accidents can only be created by new 
    or different accident initiators or sequences. This change request 
    proposes to improve the clarity of the
    
    [[Page 10399]]
    Technical Specifications requirements contained in Technical 
    Specification Section 15.3.10. The proposed specifications will 
    clarify the existing Technical Specifications where identified by 
    rewording, supplementing, or replacing existing requirements. There 
    is no physical change to the facility or its systems. Therefore, a 
    new or different kind of accident cannot occur, because no factors 
    have been introduced that could create a new or different accident 
    initiator.
        3. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The margins of safety for Point Beach are based on the design 
    and operation of the reactor and containment and the safety systems 
    that provide their protection.
        This change request proposes to improve the clarity of the 
    Technical Specifications requirements contained in Technical 
    Specification Section 15.3.10. The proposed specifications will 
    clarify the existing Technical Specifications where identified by 
    rewording, supplementing, or replacing existing requirements. There 
    is no physical change to the facility or its systems. Section 
    15.3.10 of the Technical Specifications provides the requirements 
    that limit the operation of the reactor and establish the 
    operability requirements for reactivity control by the control rod 
    system. The proposed Technical Specifications changes continue to 
    provide the appropriate limiting conditions for operation, action 
    statements, and allowable outage times that ensure the applicable 
    margins of safety to protect the reactor are preserved. Therefore, 
    no reduction in any margin of safety has been introduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power and Light Company, Docket No. 50-400, Shearon Harris 
    Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendments: February 16, 1996
        Brief description of amendments: The amendments provide a one-time 
    surveillance requirement extension for the performance of the trip 
    actuating device operational test for one of the safety injection 
    manual initiation switches.
        Date of publication of individual notice in Federal Register: 
    February 26, 1996 (61 FR 7125)
        Expiration date of individual notice: March 27, 1996
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: December 19, 1995, as 
    supplemented by letter dated February 9, 1996.
        Brief description of amendments: These amendments allow the 
    implementation of the recently approved Option B to 10 CFR Part 50, 
    Appendix J, Option B, by referring to Regulatory Guide 1.163, 
    ``Performance Based Containment Leakage - Test Program.'' This new rule 
    allows a performance-based option for determining the test frequency 
    for containment leakage rate testing. The amendment would modify 
    Technical Specifications (TS) 1.7, 3/4.6.1.1, 3/4.6.1.2, 3/4.6.1.3, and 
    3/4.6.3, and the Bases of TS 3/4.6.1.2, and would add a new TS 6.16.
        Date of issuance: February 23, 1996
        Effective date: February 23, 1996, to be implemented within 15 days 
    of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 103; Unit 2 - Amendment No. 
    92; Unit 3 - Amendment No. 75.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1627) The February 9, 1996, supplemental letter provided clarifying 
    information and did not change the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated February 23, 
    1996.No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
    
    [[Page 10400]]
    
    
    Baltimore Gas and Electric Company, Docket No. 50-317, Calvert 
    Cliffs Nuclear Power Plant, Unit No. 1, Calvert County, Maryland
    
        Date of application for amendment: December 21, 1995
        Brief description of amendment: The amendment allows the use of 
    cladding material other than Zircaloy or ZIRLO. The Safety Evaluation 
    addresses the safety significance of loading four (4) lead fuel 
    assemblies (LFAs) into the Calvert Cliffs Nuclear Power Plant, Unit No. 
    1, reactor vessel during cycles 13, 14, and 15. A Temporary Exemption 
    was issued on November 28, 1995, (60 FR 62483) approving the loading of 
    the 4 LFAs into the Unit 1 reactor vessel for the cycles noted above. 
    The technical basis for the Temporary Exemption, which is the same 
    basis for the requested TS amendment, was provided in the Baltimore Gas 
    and Electric Company submittal dated July 13, 1995.
        Date of issuance: February 21, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 211
        Facility Operating License No. DPR-53: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1627) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 21, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Units 1 and 2, Ogle County, IllinoisDocket Nos. STN 
    50-456 and STN 50-457, Braidwood Station, Units 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: June 8, 1995
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) 3/4.8.1 by (1) replacing Table 4.8-1, ``Diesel 
    Generator Test Schedule,'' with a single surveillance interval of at 
    least once per 31 days, and (2) deleting TS 4.8.1.1.3, ``Reports.'' The 
    amendments also revise ACTION statements and surveillances in TS 
    3.8.1.1 related to certain diesel generator testing and startup 
    requirements.Date of issuance: February 16, 1996Effective date: 
    Immediately, to be implemented within 90 days.
        Amendment Nos.: 79 and 71
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45176) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 16, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: June 8, 1995
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) 3/4.8.1 by (1) replacing Table 4.8.1.1.2-1, ``Diesel 
    Generator Test Schedule,'' with a single surveillance interval of at 
    least once per 31 days, and (2) deleting TS 4.8.1.1.3, ``Reports.'' The 
    amendments also revise ACTION statements and surveillances in TS 
    3.8.1.1 related to certain diesel generator testing and startup 
    requirements.
        Date of issuance: February 16, 1996
        Effective date: Immediately, to be implemented within 90 days.
        Amendment Nos.: 109 and 94
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45176) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 16, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois alley Community College, Oglesby, Illinois 61348.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Unit No. 3 Nuclear Generating Plant, Citrus County, Florida
    
        Date of application for amendment: November 3, 1995
        Brief description of amendment: This amendment allows deferral of 
    the Reactor Coolant Pump flywheel inspection until outage 11, scheduled 
    for the spring of 1998.
        Date of issuance: February 15, 1996
        Effective date: February 15, 1996
        Amendment No.: 153
        Facility Operating License No. DPR-72. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65679) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 15, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: May 5, 1995, as supplemented by 
    letter dated September 28, 1995
        Brief description of amendments: The amendments consist of changes 
    to the Technical Specifications (TS) relating to implementation of a 
    revised thermal design procedure and steam generator water level low-
    low setpoint
        Date of issuance: February 20, 1996
        Effective date: February 20, 1996
        Amendment Nos.: 183 and 177Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: October 25, 1995 (60 FR 
    54719) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 20, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 22, 1995, as supplemented by letter 
    dated October 9, 1995.
        Brief description of amendments: The amendments revised Technical 
    Specification 4.8.1.1.2.e.7 to allow the performance of the 24-hour 
    surveillance test of the diesel generators during power operation.Date 
    of issuance: February 21, 1996Effective date: February 21, 1996, to be 
    implemented within 30 days of issuance.
    
    [[Page 10401]]
    
        Amendment Nos.: Unit 1 - Amendment No. 81; Unit 2 - Amendment No. 
    70
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37091) The October 9, 1995, supplement provided clarifying information 
    and did not change the original no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 21, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: October 27, 1995
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.1.3, ``Control Rod OPERABILITY,'' to include the 
    25% surveillance overrun allowed by Limiting Condition for Operation 
    (LCO) 3.0.2 into the allowances of the surveillance Notes for control 
    rod ``notch'' testing per Surveillance Requirement (SR) 3.1.3.2 and SR 
    3.1.3.3. The amendment also includes a clarification to the description 
    of TS Table 3.3.3.1-1, ``Post Accident Monitoring Instrumentation,'' 
    Function 7, to indicate that the Function's requirements apply to the 
    position indication for only automatic primary containment isolation 
    valves, rather than all primary containment isolation valves. Finally, 
    the amendment includes changes to correct a number of editorial and 
    typographical errors inadvertently contained in TS 3.3.4.1, ``End of 
    Cycle Recirculation Pump Trip (EOC-RPT) Instrumentation,'' TS 3.3.6.1, 
    ``Primary Containment and Drywell Isolation Instrumentation,'' TS 
    3.3.8.2, ``Reactor Protection System (RPS) Electric Power Monitoring,'' 
    and TS 3.6.5.2, ``Drywell Air Lock.''
        Date of issuance: February 29, 1996
        Effective date: February 29, 1996
        Amendment No.: 102
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65680) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 29, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: August 30, 1995, as supplemented 
    by letter dated January 15, 1996.
        Brief description of amendment: The amendment revises Technical 
    Specification 1.3, ``Reactor'', to (1) allow the use of fuel rods clad 
    with Zircaloy or ZIRLO, rather than restrict use to fuel rods clad with 
    Zircaloy-4, and (2) replace the specified enrichment limit with a 
    limitation similar to that found in NUREG-1432, ``Standard Technical 
    Specifications for Combustion Engineering Plants.''
        Date of issuance: February 29, 1996
        Effective date: As of the date of issuance, to be implemented 
    concurrent with Amendment No. 144.
        Amendment No.: 155
        Facility Operating License No. DPR-36: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 11, 1995 (60 FR 
    52932) The January 15, 1996, submittal provided clarifying information 
    and did not change the initial proposed no significant hazards 
    determination.The Commission's related evaluation of the amendment is 
    contained in Safety Evaluation dated February 29, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578.
    
    Niagara Mohawk Power Corporation, Docket Nos. 50-220, and 50-410, 
    Nine Mile Point Nuclear Station, Unit Nos. 1 and 2, Oswego County, 
    New York
    
        Date of application for amendments: October 25, 1995, as 
    supplemented February 7, 1996.
        Brief description of amendments: The amendments revise portions of 
    Chapter 6 of the Technical Specifications to reflect management 
    position title and responsibility changes.Date of issuance: February 
    20, 1996
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment Nos.: 157 and 71
        Facility Operating License Nos. DPR-63 and NPF-69: Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: November 16, 1995 (60 
    FR 57605) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 20, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: August 1, 1995
        Brief description of amendments: These amendments revise the 
    Technical Specifications Section 3/4.9.1, ``Reactor Mode Switch,'' in 
    order to provide alternate actions to allow the continuation of core 
    alterations in the event certain Reactor Manual Control System (RMCS) 
    and refueling interlocks are inoperable, while preserving the intended 
    function of the inoperable interlocks.
        Date of issuance: February 23, 1996
        Effective date: As of date of issuance, to be implemented within 30 
    days.
        Amendment Nos.: 114 and 76
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49944) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 23, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: October 31, 1994
        Brief description of amendment: This amendment deletes certain 
    valves from Technical Specification Table 3.6.3-1, ``Primary 
    Containment Isolation Valves,'' that no longer need to be tested in 
    accordance with 10 CFR Part 50, Appendix J.
        Date of issuance: February 22, 1996
        
    [[Page 10402]]
    
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment No.:  93
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 29, 1995 (60 FR 
    16198) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 22, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  Pennsville Public Library, 
    190 S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: February 5, 1996, as 
    supplemented by letter dated February 14, 1996.
        Brief description of amendment: The amendment changes Technical 
    Specifications 4.6.2.2b, ``Suppression Pool Spray,'' and 4.6.2.3b, 
    ``Suppression Pool Cooling,'' to include flow through the RHR heat 
    exchanger bypass line (in addition to the RHR heat exchanger) in the 
    Suppression Pool Cooling and Suppression Pool Spray flow path used 
    during RHR pump testing.
        Date of issuance: February 26, 1996
        Effective date: As of date of issuance, to be implemented within 3 
    days.
        Amendment No.: 94
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes (61 FR 5040) February 9, 1996. 
    That notice provided an opportunity to submit comments on the 
    Commission's proposed no significant hazards consideration 
    determination. No comments have been received. The notice also provided 
    for an opportunity to request a hearing by March 11, 1996, but 
    indicated that if the Commission makes a final no significant hazards 
    consideration determination any such hearing would take place after 
    issuance of the amendment.The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated February 26, 1996.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: September 28, 1995
        Brief description of amendments: The changes relocate ``Reactor 
    Coolant System - Chemistry'' Technical Specification 3/4.4.7 for Salem 
    Unit 1 and 3/4.4.8 for Salem Unit 2 and their associated Bases to the 
    Salem Updated Final Safety Analysis Report and the Surveillance 
    Requirements and Limiting Conditions for Operations to applicable plant 
    procedures controlled by the 10 CFR 50.59 process. Also, the 
    applicability will be changed from ``At all times'' to ``Modes 1, 2, 3, 
    4, 5, and 6.''
        Date of issuance: February 22, 1996
        Effective date: Units 1 and 2, as of date of issuance and shall be 
    implemented within 60 days of date of issuance.
        Amendment Nos.: 180 and 161
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 8, 1995 (60 FR 
    56369) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 22, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
    
    Sacramento Municipal Utility District, Docket No. 50-312, Rancho 
    Seco Nuclear Generating Station, Sacramento County, California
    
        Date of application for amendment: June 20, 1995, as supplemented 
    on December 19, 1995 and February 7, 1996.
        Brief description of amendment: This amendment modifies the 
    technical specification requirements on qualifications for reviewers of 
    facility modifications, programs, and documents affecting nuclear 
    safety and changes the required schedule for reporting changes 
    requested to environmental permits.
        Date of issuance: February 26, 1996
        Effective date: February 26, 1996
        Amendment No.: 124
        Facility Operating License No. NPF-1: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37099) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 26, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Central Library, Government 
    Documents, 828 I Street, Sacramento, California 95814
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: November 20, 1995
        Brief description of amendment: The amendment adds the following 
    footnote to Technical Specification (TS) 3/4.5.2: ``The allowable 
    outage time for each RHR train may be extended to 7 days for the 
    purpose of maintenance and modification. This exception may only be 
    used one time per RHR train and is not valid after December 31, 1997.''
        Date of issuance: February 21, 1996
        Effective date: February 21, 1996
        Amendment No.: 132
        Facility Operating License No. NPF-12: Amendment revises the TS.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65684) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 21, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: October 14, 1992, as 
    supplemented by letter dated December 18, 1995
        Brief description of amendments: These amendments revise TS 3/
    4.7.5, ``Control Room Emergency Air Cleanup System,'' by reducing the 
    test duration for the control room emergency air cleanup system and 
    deleting requirements for duct heaters and diverting valves. The 
    associated Bases are also revised to reflect these changes.
        Date of issuance: February 28, 1996
        Effective date: February 28, 1996, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 128; Unit 2 - Amendment No. 
    117
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
    
    [[Page 10403]]
    
        Date of initial notice in Federal Register: March 3, 1993 (58 FR 
    12267) The December 18, 1995, supplemental letter provided additional 
    clarifying information and did not change the initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    February 28, 1996.No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments:  December 8, 1995 supplemented 
    January 10, 1996 (TS 364)
        Brief description of amendment: The amendments implement recent 
    changes to 10 CFR 50 Appendix J for performance-based testing of 
    containment leakage.
        Date of issuance: February 22, 1996
        Effective Date: February 22, 1996
        Amendment Nos.: 228, 243 and 203
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1637) The letter dated January 10, 1996 provided information that did 
    not change the initial proposed finding of no significant hazards 
    consideration. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 22, 1996.No significant 
    hazards consideration comments received: None
        Local Public Document Room location:  Athens Public library, South 
    Street, Athens, Alabama 35611
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: November 22, 1995
        Brief description of amendment: The amendment added OES Nuclear, 
    Inc. as an owner.
        Date of issuance: February 27, 1996
        Effective date: February 27, 1996
        Amendment No.: 81
        Facility Operating License No. NPF-58: This amendment revised the 
    license.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65685) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 27, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: December 12, 1995, supplemented 
    by facsimile transmission dated January 26, 1996
        Brief description of amendment: This amendment revises TS 3/
    4.6.1.1, Containment Systems - Primary Containment -Containment 
    Integrity; TS 3/4.6.1.2, Containment Systems - Containment Leakage; TS 
    3/4.6.1.6, Containment Systems - Containment Vessel Structural 
    Integrity; TS 3/4.6.5.3, Containment Systems - Shield Building 
    Structural Integrity; and associated Bases. The revisions incorporate 
    changes to the TS to adopt the provisions of Appendix J, Option B for 
    Type A containment leakage testing as modified by approved exemptions 
    and in accordance with Regulatory Guide 1.163, to provide consistency 
    with these new requirements, and to make administrative changes.
        Date of issuance: February 22, 1996
        Effective date: February 22, 1996, and implemented not later than 
    90 days after issuance.
        Amendment No.: 205
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1637) The January 26, 1996, facsimile transmission was clarifying in 
    nature and did not affect the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated February 22, 
    1996.No significant hazards consideration comments received: No.
        Local Public Document Room location:  University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: June 1, 1995, as supplemented on 
    October 20, 1995, December 13, 1995, and January 26, 1996.
        Brief description of amendment: The amendment revised the allowed 
    outage time for one unavailable emergency diesel generator from 72 
    hours to 7 days.
        Date of issuance: February 26, 1996
        Effective date: February 26, 1996
        Amendment No.: 206
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 2, 1995 (60 FR 
    39453) Supplemental information submitted on October 20, 1995, December 
    13, 1995, and January 26, 1996, provided clarification only and was not 
    outside the scope of the original no significant hazards determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated February 26, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: September 29, 1995
        Brief description of amendment: The amendment increases the minimum 
    available borated water volume requirement for the boric acid addition 
    system, the minimum and maximum boron concentration requirements for 
    the borated water storage tank, the minimum boron concentration 
    requirement for the core flood tanks; modifies the surveillance 
    requirements for trisodium phosphate dodecahydrate; and modifies the 
    refueling boron concentration and the associated Action statement.
        Date of issuance: February 27, 1996
        Effective date: February 27, 1996
        Amendment No.: 207
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 8, 1995 (60 FR
    
    [[Page 10404]]
    56371) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 27, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: November 29, 1994
        Brief description of amendments: The amendments revise and update 
    the North Anna Units 1 and 2 Environmental Protection Plan (EPP) to 
    reflect current obligations to the Commonwealth of Virginia, revise 
    portions of the transmission corridor rights-of-way erosion control 
    program for clarification and to be consistent with the state 
    regulations, eliminate inconsistencies, and delete obsolete material.
        Date of issuance: February 20, 1996
        Effective date: February 20, 1996
        Amendment Nos.: 197 and 198
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45188) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 20, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments:  October 17, 1995, as 
    supplemented by facsimile dated February 26, 1996.
        Brief description of amendments: The amendments revise the North 
    Anna Units 1 and 2 Technical Specifications (TS) to allow both of the 
    containment personnel airlock doors to remain open during refueling 
    operations, delete License Condition 2.G for Unit 1 and 2.I for Unit 2, 
    which reference the analyses for limiting doses to control room 
    operators, and modify the TS Bases to clarify the emergency power 
    system requirements relative to mitigation of the consequences of a 
    Fuel Handling Accident.
        Date of issuance: February 27, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: Unit 1 - 198; Unit 2 -179
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications and License Conditions.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    187) The February 26, 1996, facsimile provided clarifying information 
    that did not change the scope of the October 17, 1995, application and 
    the initial proposed no significant hazards consideration 
    determination.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 27, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: November 22, 1995, as supplemented by 
    letter dated February 8, 1996.
        Brief description of amendment: This amendment allows the personnel 
    airlock doors to be open during core alterations and movement of 
    irradiated fuel in containment. The surveillance requirements for 
    containment penetrations have also been revised to require that each be 
    in its ``required condition'' instead of ``closed/isolated condition.'' 
    The Bases section has been updated.
        Date of issuance: February 28, 1996
        Effective date: February 28, 1996, to be implemented within 30 days 
    of issuance.
        Amendment No.: Amendment No. 95
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65687) The February 8, 1996, supplemental letter provided additional 
    clarifying information and did not change the original no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    February 28, 1996.No significant hazards consideration comments 
    received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards
    
    [[Page 10405]]
    consideration determination. In such case, the license amendment has 
    been issued without opportunity for comment. If there has been some 
    time for public comment but less than 30 days, the Commission may 
    provide an opportunity for public comment. If comments have been 
    requested, it is so stated. In either event, the State has been 
    consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By April 12, 1996, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 2.714, a petition for leave to intervene shall 
    set forth with particularity the interest of the petitioner in the 
    proceeding, and how that interest may be affected by the results of the 
    proceeding. The petition should specifically explain the reasons why 
    intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the
    
    [[Page 10406]]
    Commission, the presiding officer or the Atomic Safety and Licensing 
    Board that the petition and/or request should be granted based upon a 
    balancing of the factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 
    2.714(d).
    
    Tennesse Valley Authority, Docket No. 50-390, Watts Bar Nuclear 
    Plant, Unit No. 1, Rhea County, Tennessee
    
        Date of application for amendment: February 26, 1996
        Brief description of amendment: The proposed amendment revises 
    Technical Specifications (TS) to allow implementation of a proposed 
    plant modification to preclude inadvertent transfer of the turbine-
    driven auxiliary feedwater pump suction from the condensate storage 
    tank to the emergency raw cooling water system.
        Date of issuance: February 28, 1996
        Effective date: February 28, 1996
        Amendment No.: 1
        Facility Operating License No. NPF-90: Amendment revises the TS. 
    The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration, are contained in a Safety Evaluation dated 
    February 28, 1996.Public comments requested as to proposed no 
    significant hazards consideration: No
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
        Dated at Rockville, Maryland, this 6th day of March 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation
    [Doc. 96-5817 Filed 3-12-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
03/13/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-10313
Dates:
February 23, 1996, to be implemented within 15 days of issuance.
Pages:
10391-10406 (16 pages)
PDF File:
x96-10313.pdf