X95-60315. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 60, Number 50 (Wednesday, March 15, 1995)]
    [Notices]
    [Pages 14015-14040]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X95-60315]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from February 16, 1995, through March 3, 1995. 
    The last biweekly notice was published on March 1, 1995.
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By April 14, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above. [[Page 14016]] 
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: January 31, 1995
        Description of amendments request: The proposed amendments would 
    revise the Technical Specifications (TSs) for Calvert Cliffs, Unit Nos. 
    1 and 2, to increase the amount of Trisodium Phosphate Dodecahydrate 
    (TSP) located in the containment sump baskets required to be verified 
    by TS surveillance. The requested change is the result of an reanalysis 
    of the amount of TSP necessary to maintain the appropriate pH in the 
    containment sump water subsequent to a Loss of Coolant Accident. 
    Specifically, the request would change the TS value of TS 4.5.2.e.3 
    from the existing amount of 100 ft3 to 289 ft3. TS 4.5.2.e.4 
    would also be changed by moving the amounts of TSP and refueling water 
    storage tank water to be used in the required tests to the TS Bases 
    Section 3/4.5.2 and 3/4.5.3. These Bases sections would also be changed 
    by modifying the test methods.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability 
    orconsequences of an accident previously evaluated.
        Trisodium Phosphate Dodecahydrate (TSP) is stored in the 
    containment lower level to raise the pH of the sump and spray water 
    following a Loss of Coolant Accident (LOCA). As the pH of the water 
    increases, more radioactive iodine is kept in solution and the 
    possibility of airborne radioactivity leakage is decreased. An 
    additional advantage of a higher pH is the beneficial reduction in 
    chloride stress corrosion cracking of metal components in the 
    containment following an accident.
        This chemical is an accident mitigator, not an accident 
    initiator in that it is not used until after an accident has 
    occurred. At the time it goes into solution, the accident has 
    occurred, containment spray has been activated and water has 
    collected in the containment sump. Therefore, increasing the 
    Technical Specification minimum amount verified to be in each 
    containment will not involve a significant increase in the 
    probability of an accident previously evaluated.
        Updated Final Safety Analysis Report, Chapter 14.24, ``Maximum 
    Hypothetical Accident'', uses an assumption of a pre-RAS minimum 
    containment spray pH of 5.0 for the iodine removal calculation and a 
    post-RAS sump pH of 7.0 for iodine retention. Raising the pH to 7.0 
    does not increase the consequences of an accident previously 
    evaluated.
        The proposed change to Technical Specification 4.5.2.e.4 would 
    remove the amounts of chemical and water used in the test to the 
    Bases. This relocation will not alter the test method or acceptance 
    criteria, but will allow adjustments to the ratio of TSP and borated 
    water under the controls of 10 CFR 50.59 to reflect changes in plant 
    conditions. In the Bases, the amount of TSP used in the test is 
    changed to reflect the ratio of TSP to water that would be found in 
    the containment following a LOCA. The specified concentration of 
    boron in the test reflects the highest concentration that could be 
    found in the containment following a LOCA. The test temperature is 
    changed to 120 deg.F which is well below the temperature expected to 
    be found in the containment sump following a LOCA. The decanting of 
    the solution does not change the intent of the test method since the 
    dissolving period will still be conducted without agitation.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated. [[Page 14017]] 
        The addition of more TSP does not represent a significant change 
    in the configuration or operation of the plant. Trisodium Phosphate 
    Dodecahydrate is currently present in the containment lower level. 
    There are no physical changes which result from the increase in 
    volume. The proposed change to Technical Specification 4.5.2.e.4 
    would move the amounts of chemical and water used in the test to the 
    Bases. This relocation will not alter the test method or acceptance 
    criteria, but will allow adjustments to the ratio of TSP and borated 
    water under the controls of 10 CFR 50.59 to reflect changes in plant 
    conditions. In the Bases, the amount of TSP used in the test is 
    changed to reflect the ratio of TSP to water that would be found in 
    the containment following a LOCA. The specified concentration of 
    boron in the test reflects the highest concentration that could be 
    found in the containment following a LOCA. The test temperature is 
    changed to 120 deg.F which is well below the temperature expected to 
    be found in the containment sump following a LOCA. The decanting of 
    the solution does not change the intent of the test method since the 
    dissolving period will still be conducted without agitation.
        Therefore, this change would not create the possibility of a new 
    or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        Trisodium Phosphate Dodecahydrate is stored in the containment 
    lower level to raise the pH of the sump and spray water following a 
    LOCA. As the pH of the water increases, more radioactive iodine is 
    kept in solution and the possibility of airborne radioactivity 
    leakage is decreased. Additionally, a higher pH has a beneficial 
    effect on chloride stress corrosion cracking of metal components in 
    the containment.
        Technical Specification 4.5.2.e.3 requires verification that a 
    minimum volume of TSP is contained in the storage baskets in each 
    containment. This change proposes to increase that volume. The 
    increased volume will ensure the containment sump, when filled with 
    water, will have an acceptable pH following a LOCA.
        The proposed change to Technical Specification 4.5.2.e.4 would 
    move the amounts of chemical and water used in the test to the 
    Bases. This relocation will not alter the test method or acceptance 
    criteria, but will allow adjustments to the ratio of TSP and borated 
    water under the controls of 10 CFR 50.59 to reflect changes in plant 
    conditions. In the Bases, the amount of TSP used in the test is 
    changed to reflect the ratio of TSP to water that would be found in 
    the containment following a LOCA. The specified concentration of 
    boron in the test reflects the highest concentration that could be 
    found in the containment following a LOCA. The test temperature is 
    changed to 120 deg.F which is well below the temperature expected to 
    be found in the containment sump following a LOCA. The decanting of 
    the solution does not change the intent of the test method since the 
    dissolving period will still be conducted without agitation.
        Therefore, this change would not involve a significant reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: February 9, 1995
        Description of amendment request: The proposed amendment would 
    increase the Reactor High Water Level Trip Level Setting for the Group 
    1 isolation. The change will allow an increase to the main steam 
    isolation valve (MSIV) high water level isolation setpoint.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        In accordance with 10 CFR 50.91, Boston Edison submits the 
    following analysis addressing the no significant hazards 
    consideration. The proposed changes do not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Operation of the station in accordance with the proposed Trip 
    Level Setting will not significantly increase the probability or 
    consequences of an accident previously evaluated. The MSIV high 
    water level isolation signal is provided to protect against rapid 
    depressurization due to a pressure regulator malfunction during 
    plant startup. The high water level isolation signal is not 
    functional when the mode switch is in the RUN position. A high water 
    level in the reactor vessel indicates that fuel is covered. 
    Increasing the Trip Level Setting will have minimal effect on 
    moisture carryover in the event of a pressure regulator failure at 
    low reactor power. MSIV closure (Group 1) is initiated by low 
    reactor pressure (810 psig) approximately 30 seconds into the event. 
    The resulting reactor water level swell is not sufficient to reach 
    the bottom elevation of the main steam lines.
        The proposed Technical Specification allowable value for the 
    Reactor Low Level Trip Level Setting and the Reactor Low Low Water 
    Level Trip Level setting does not involve significant increase in 
    the probability or consequence of an accident.
        (2) Create the possibility of a new or different kind of 
    accident from any previously analyzed.
        The proposed change does not affect the Group 1 isolation safety 
    function. The change does not involve any plant hardware changes 
    that could introduce any new failure modes or effects; thus, the 
    change can not create the possibility of a new or different kind of 
    accident from any previously analyzed.
        (3) Involve a significant reduction in a margin of safety.
        The proposed change does not affect the Group 1 isolation safety 
    function. The proposed change is consistent with the FSAR [Final 
    Safety Analysis Report] and Technical Specification basis associated 
    with reactor vessel inventory control and main steam line flooding.
        The proposed change to the instrument calibration range does not 
    affect the margin of safety for systems or components affected by 
    the change. Operating Pilgrim in accordance with the proposed Trip 
    Level Setting does not involve a significant reduction in the margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Walter R. Butler
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: February 6, 1995
        Description of amendment request: The change proposes to relocate 
    the cycle specific core operating limits of Figure 3.1-1, Shutdown 
    Margin Versus Boron Concentration, from Technical Specification (TS) 
    3.1.1.2, Shutdown Margins - Modes 3, 4, and 5, to the Core Operating 
    Limits Report (COLR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change of relocating TS Figure 3.1-1, Shutdown 
    Margin Versus Boron Concentration to the COLR has no influence 
    [[Page 14018]] or impact to the probability or consequences of an 
    accident. The revised TS will continue to implement the shutdown 
    margin limits through reference to the Shutdown Margin Curve in the 
    COLR. In addition, the COLR is subject to the existing controls of 
    TS 6.9.1.6. Given that this change is an administrative relocation 
    of the Shutdown Margin Curve to another TS controlled document, 
    there would be no increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        No safety-related equipment, safety function, or plant operation 
    will be altered as a result of this proposed change. The TS will 
    continue to require operation within the required core operating 
    limits. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        Relocation of the Shutdown Margin Curve to the TS controlled 
    COLR has no effect on the core operating limits currently in force 
    in TS 3.1.1.2. Future revisions to the Shutdown Margin Curve are 
    governed by TS 6.9.1.6 which stipulates the specific TS that 
    reference the COLR limits and the methodologies utilized in 
    developing those limits. Given that the change is an administrative 
    relocation of the Shutdown Margin Curve to another TS controlled 
    document, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: William H. Bateman
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: January 12, 1995
        Description of amendment request: The proposed amendments would 
    revise and clarify portions of Technical Specification (TS) Section 
    6.0, ``Administrative Controls,'' for the McGuire, Catawba, and Oconee 
    nuclear stations. The licensee submitted a combined amendment request 
    covering the three Duke Power nuclear stations. The proposed changes 
    are described below.
        1. Remove the specific assignment of responsibilities for the 
    review, distribution, and approval activities contained in the 
    Technical Review and Control Section of each station's TS. The proposed 
    specifications state that these activities will be performed by a 
    knowledgeable individual/organization. Approval of the affected 
    documents is to be at the appropriate manager/superintendent level as 
    specified in Duke administrative controls.
        2. Move the requirement for the review of proposed changes in the 
    stations' TS and Operating Licenses by the Duke Nuclear Safety Review 
    Board (NSRB) to Duke administrative procedures (Selected Licensee 
    Commitments documents) and change the wording of the requirements 
    covering NSRB meeting frequency. The Oconee TS covering the NSRB are 
    being rewritten to be consistent with McGuire and Catawba.
        3. Add Technical Review and Control Program implementation and 
    Plant Operations Review Committee (PORC) implementation to the list of 
    required procedures and programs for each nuclear station.
        4. Change or clarify certain TS administrative requirements 
    covering technical review and control activities or records retention 
    requirements.
        5. For Oconee only, under ``Station Operating Procedures,'' revise 
    the TS requirements covering the review and approval of station 
    procedures and temporary procedure changes such that these are now 
    consistent with the corresponding requirements for McGuire and Catawba.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (It should be noted that the licensee submitted a combined 
    analysis that covers McGuire, Catawba, and Oconee nuclear stations.)
        Standard 1. The proposed amendments will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The provisions of these proposed amendments concern 
    administrative changes in the stations' Technical Specifications 
    involving the Technical Review and Control, Procedures and Programs/
    Station Operating Procedures, and Records Retention/Station 
    Operating Records portions of the Administrative Controls Section. 
    The requested changes primarily affect review and control 
    activities, but also include other administrative changes affecting 
    the approval of station procedures (Oconee only), records retention, 
    and definition of the term ODCM [offsite dose calculation manual] 
    (McGuire and [Catawba]). The provisions of the proposed amendment 
    primarily involve the relocation of existing Technical 
    Specifications review, distribution, or approval requirements to 
    internal Duke administrative controls. However, implementation of 
    the proposed amendment does involve changes to several review/
    distribution activities. Theses review/distribution activities are 
    primarily for: 1) Proposed changes to the stations' Technical 
    Specifications, 2) Proposed tests and experiments which affect 
    nuclear safety and are not addressed in the stations' FSAR [Final 
    Safety Analysis Report] or Technical Specifications, 3) 
    Environmental radiological procedures, 4) Reportable events 
    documentation and reports of violations of Technical Specifications, 
    5) Reports of special reviews and investigations, and 6) Reports of 
    unplanned onsite releases of radiological material to the environs. 
    Planned implementation of the proposed Technical Specifications 
    amendments utilizing Selected Licensee Commitments will result in 
    the above items being reviewed/received by a different 
    organizational unit in the future. The organizational unit is to be 
    either the recently initiated Plant Operations Review Committee 
    (PORC) or the General Manager, Environmental Services. Personnel 
    serving on the PORC, and the General Manager, Environmental Services 
    will be qualified based upon education and experience to review the 
    operational and technical considerations involved with the 
    applicable items listed above. No required reviews are being 
    eliminated by the requested amendments, only the organizational 
    units responsible for performing the reviews will be changed. Future 
    reviews of theses items under the auspices of the PORC or the 
    General Manager, Environmental Services will maintain a quality 
    level equivalent to that being currently achieved by Duke's 
    Qualified Reviewer Program, the Station Managers, or the
        Duke Nuclear Safety Review Board as applicable. Consequently, 
    merely changing the organizational units performing future reviews, 
    or making the additional administrative changes described above, 
    results in no increase in the probability or consequences of an 
    accident previously evaluated because the review function will 
    continue to be conducted in an equivalent manner.
        The implementing SLC will also permit proposed amendments to the 
    stations' Technical Specifications and Operating Licenses to be 
    approved for the Station Manager by a designee. However, this 
    individual will occupy a position equivalent to, or higher, in the 
    Duke organization as the Station manager.
        Additionally, the proposed changes do not directly impact the 
    design or operation of any plant systems or components any more so 
    than the review and approval processes currently being conducted in 
    accordance [[Page 14019]] with existing approved Technical 
    Specifications.
        Standard 2. The proposed amendments will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The proposed changes are administrative in nature and primarily 
    cover the review, distribution, and/or approval function performed 
    for items identified in existing Technical Specifications. The 
    quality level of the future reviews will not decrease and the 
    ability of Duke to identify the possibility for the concurrence of 
    new or different kinds of accidents prior to implementation will be 
    maintained. Of specific interest in the consideration of Standard 
    2 is the review of proposed tests and experiments which 
    affect station nuclear safety and are not addressed in the FSAR or 
    Technical Specifications. The Technical Specifications required 
    reviews of these tests and experiments are not being proposed for 
    removal by these requested amendments. Only the organizational unit 
    conducting the review of proposed tests and experiments is being 
    changed by the requested amendments. The PORC, instead of the 
    Station Manager, is being assigned the responsibility for conducting 
    the reviews of proposed tests and experiments in the future. It is 
    believed that the combined expertise of the PORC membership will 
    enhance Duke's ability to identify potential situations which could 
    possibly involve a new, or different, kind of accident.
        Standard 3. The proposed amendments will not involve a 
    significant reduction in any margin of safety.
        The changes contained in the requested amendments are 
    administrative in nature and do not impact the design capabilities 
    or operation of any plant structures, systems, or components. There 
    will be no reduction in margin of safety as a result of implementing 
    these requested amendments. Impact upon margin of safety is a 
    consideration primarily included in the 10 CFR 50.59 evaluation 
    process conducted for station procedures, procedure changes, and 
    nuclear station modifications. The 10 CFR 50.59 evaluation process 
    in conducted under the auspices of the Duke Qualified Reviewer 
    Program and is not affected by these requested amendments. The 
    impact on margin of safety for future Technical Specifications and 
    Operating License changes will be reviewed by the PORC, but these 
    reviews will be equivalent in quality to the reviews presently 
    conducted by the Qualified Reviewers.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: January 13, 1995
        Description of amendment request: The proposed amendments would 
    increase the surveillance test intervals and allowed outage times for 
    Reactor Trip System (RTS) and Engineered Safety Features Actuation 
    System (ESFAS) equipment based upon analyses by Westinghouse for the 
    Westinghouse Owners Group and approved by the NRC. The proposed changes 
    to the RTS and ESFAS instrumentation are based upon WCAP-10271, its 
    supplements, and the NRC's safety evaluation reports.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1 - Operation of McGuire in accordance with the 
    proposed license amendment[s] [do] not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The determination that the results of the proposed changes are 
    within all acceptable criteria was established in the SERs prepared 
    for WCAP-10271, WCAP-10271 Supplement 1, WCAP-10271 Supplement 2, 
    and WCAP-10271 Supplement 2, Revision 1 issued by letters dated 
    February 21, 1985, February 22, 1989, and April 30, 1990. 
    Implementation of the proposed changes is expected to result in an 
    acceptable increase in total RTS yearly unavailability. This 
    increase, which is primarily due to less frequent surveillance, 
    results in an increase of similar magnitude in the probability of an 
    Anticipated Transient Without Scram (ATWS) and in the probability of 
    core melt resulting from an ATWS and also results in a small 
    increase in core damage frequency (CDF) due to ESFAS unavailability.
        Implementation of the proposed changes is expected to result in 
    a significant reduction in the probability of core melt from 
    inadvertent reactor trips. This is a result of a reduction in the 
    number of inadvertent reactor trips (0.5 fewer inadvertent reactor 
    trips per unit per year) occurring during testing of RTS 
    instrumentation. This reduction is primarily attributable to testing 
    in bypass and less frequent surveillance.
        The reduction in core melt frequency from inadvertent reactor 
    trips is sufficiently large to counter the increase in ATWS core 
    melt probability resulting in an overall reduction in total core 
    melt probability.
        The values determined by the WOG and presented in the WCAP for 
    the increase in CDF were verified by Brookhaven National Laboratory 
    (BNL) as part of an audit and sensitivity analysis for the NRC 
    staff. Based on the small value of the increase compared to the 
    range of uncertainty in the CDF, the increase is considered 
    acceptable.
        Changes to surveillance test frequencies for the RTS [reactor 
    trip system] interlocks do not represent a significant reduction in 
    testing. The currently specified test interval for interlock 
    channels allows the surveillance requirement to be satisfied by 
    verifying that the permissive logic is in its required state using 
    the permissive annunciator window. The surveillance as currently 
    required only verifies the status of the permissive logic and does 
    not address verification of channel setpoint or operability. The 
    setpoint verification and channel operability are verified after a 
    refueling shutdown. The definition of the channel check includes 
    comparison of the channel status with other channels for the same 
    parameter. The requirement to routinely verify permissive status is 
    a different consideration than the availability of trip or actuation 
    channels which are required to change state on the occurrence of an 
    event and for which the function availability is more dependent on 
    the surveillance interval. The change in surveillance requirement to 
    at least once every refueling does not therefore represent a 
    significant change in channel surveillance and does not involve a 
    significant increase in unavailability of the RTS.The proposed 
    changes do not result in an increase in the severity or consequences 
    of an accident previously evaluated. Implementation of the proposed 
    changes affects the probability of failure of the RTS but does not 
    alter the manner in which protection is afforded nor the manner in 
    which limiting criteria are established.
        Criterion 2 - The proposed license amendment[s] [do] not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        The proposed changes do not result in a change in the manner in 
    which the RTS provides plant protection. No change is being made 
    which alters the functioning of the RTS (other than in a test mode). 
    Rather, the likelihood or probability of the RTS functioning 
    properly is affected as described above. Therefore, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident.
        The proposed changes do not involve hardware changes except 
    those necessary to implement testing in bypass. Some existing 
    instrumentation is designed to be tested in bypass and current 
    Technical Specifications allow testing in bypass. Testing in bypass 
    is also recognized by IEEE standards. Therefore, testing in bypass 
    has been previously approved and implementation of the proposed 
    changes for testing in bypass does not create the possibility of a 
    new or different kind of accident from any previously evaluated. 
    Furthermore, since the other proposed changes do not alter the 
    functioning of the RTS, the possibility of a new or different kind 
    of accident from any previously evaluated has not been created.
        Criterion 3 - The proposed license amendment[s] [do] not involve 
    a significant reduction in a margin of safety.
        The proposed changes do not alter the manner in which safety 
    limits, limiting safety [[Page 14020]] system setpoints, or limiting 
    conditions for operation are determined. The impact of reduced 
    testing other than as addressed above is to allow a longer time 
    interval over which instrument uncertainties (e.g., drift) may act. 
    Experience has shown that the initial uncertainty assumptions are 
    valid for reduced testing.
        Implementation of the proposed changes is expected to result in 
    an overall improvement in safety by:
        1) Less frequent testing will result in fewer inadvertent 
    reactor trips and actuation of Engineered Safety Features Actuation 
    System components.
        2) Higher quality repairs leading to improved equipment 
    reliability due to longer allowable repair times.
        3) Improvements in the effectiveness of the operating staff in 
    monitoring and controlling plant operation. This is due to less 
    frequent distraction of the operator and shift supervisor to attend 
    to instrumentation testing.
        The foregoing analysis demonstrates that the proposed 
    amendment[s] to McGuire's Technical Specifications [do] not involve 
    a significant increase in the probability or consequences of a 
    previously evaluated accident, [do] not create the possibility of a 
    new or different kind of accident, and [do] not involve a 
    significant reduction in a margin of safety.
        Based upon the preceding analysis, Duke Power Company concludes 
    that the proposed amendment[s] [do] not involve a significant 
    hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: January 12, 1995
        Description of amendment request: The proposed amendments would 
    revise and clarify portions of Technical Specification (TS) Section 
    6.0, ``Administrative Controls,'' for the McGuire, Catawba, and Oconee 
    nuclear stations. The licensee submitted a combined amendment request 
    covering the three Duke Power nuclear stations. The proposed changes 
    are described below.
        1. Remove the specific assignment of responsibilities for the 
    review, distribution, and approval activities contained in the 
    Technical Review and Control Section of each station's TS. The proposed 
    specifications state that these activities will be performed by a 
    knowledgeable individual/organization. Approval of the affected 
    documents is to be at the appropriate manager/superintendent level as 
    specified in Duke administrative controls.
        2. Move the requirement for the review of proposed changes in the 
    stations' TS and Operating Licenses by the Duke Nuclear Safety Review 
    Board (NSRB) to Duke administrative procedures (Selected Licensee 
    Commitments documents) and change the wording of the requirements 
    covering NSRB meeting frequency. The Oconee TS covering the NSRB are 
    being rewritten to be consistent with McGuire and Catawba.
        3. Add Technical Review and Control Program implementation and 
    Plant Operations Review Committee (PORC) implementation to the list of 
    required procedures and programs for each nuclear station.
        4. Change or clarify certain TS administrative requirements 
    covering technical review and control activities or records retention 
    requirements.
        5. For Oconee only, under ``Station Operating Procedures,'' revise 
    the TS requirements covering the review and approval of station 
    procedures and temporary procedure changes such that these are now 
    consistent with the corresponding requirements for McGuire and Catawba.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (It should be noted that the licensee submitted a combined 
    analysis that covers McGuire, Catawba, and Oconee nuclear stations.)
        Standard 1. The proposed amendments will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The provisions of these proposed amendments concern 
    administrative changes in the stations' Technical Specifications 
    involving the Technical Review and Control, Procedures and Programs/
    Station Operating Procedures, and Records Retention/Station 
    Operating Records portions of the Administrative Controls Section. 
    The requested changes primarily affect review and control 
    activities, but also include other administrative changes affecting 
    the approval of station procedures (Oconee only), records retention, 
    and definition of the term ODCM [offsite dose calculation manual] 
    (McGuire and [Catawba]). The provisions of the proposed amendment 
    primarily involve the relocation of existing Technical 
    Specifications review, distribution, or approval requirements to 
    internal Duke administrative controls. However, implementation of 
    the proposed amendment does involve changes to several review/
    distribution activities. These review/distribution activities are 
    primarily for: 1) Proposed changes to the stations' Technical 
    Specifications, 2) Proposed tests and experiments which affect 
    nuclear safety and are not addressed in the stations' FSAR [Final 
    Safety Analysis Report] or Technical Specifications, 3) 
    Environmental radiological procedures, 4) Reportable events 
    documentation and reports of violations of Technical Specifications, 
    5) Reports of special reviews and investigations, and 6) Reports of 
    unplanned onsite releases of radiological material to the environs. 
    Planned implementation of the proposed Technical Specifications 
    amendments utilizing Selected Licensee Commitments will result in 
    the above items being reviewed/received by a different 
    organizational unit in the future. The organizational unit is to be 
    either the recently initiated Plant Operations Review Committee 
    (PORC) or the General Manager, Environmental Services. Personnel 
    serving on the PORC, and the General Manager, Environmental Services 
    will be qualified based upon education and experience to review the 
    operational and technical considerations involved with the 
    applicable items listed above. No required reviews are being 
    eliminated by the requested amendments, only the organizational 
    units responsible for performing the reviews will be changed. Future 
    reviews of these items under the auspices of the PORC or the General 
    Manager, Environmental Services will maintain a quality level 
    equivalent to that being currently achieved by Duke's Qualified 
    Reviewer Program, the Station Managers, or the Duke Nuclear Safety 
    Review Board as applicable. Consequently, merely changing the 
    organizational units performing future reviews, or making the 
    additional administrative changes described above, results in no 
    increase in the probability or consequences of an accident 
    previously evaluated because the review function will continue to be 
    conducted in an equivalent manner.
        The implementing SLC will also permit proposed amendments to the 
    stations' Technical Specifications and Operating Licenses to be 
    approved for the Station Manager by a designee. However, this 
    individual will occupy a position equivalent to, or higher, in the 
    Duke organization as the Station Manager.
        Additionally, the proposed changes do not directly impact the 
    design or operation of any plant systems or components any more so 
    than the review and approval processes currently being conducted in 
    accordance with existing approved Technical Specifications.
        Standard 2. The proposed amendments will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The proposed changes are administrative in nature and primarily 
    cover the review, [[Page 14021]] distribution, and/or approval 
    function performed for items identified in existing Technical 
    Specifications. The quality level of the future reviews will not 
    decrease and the ability of Duke to identify the possibility for the 
    occurrence of new or different kinds of accidents prior to 
    implementation will be maintained. Of specific interest in the 
    consideration of Standard 2 is the review of proposed tests 
    and experiments which affect station nuclear safety and are not 
    addressed in the FSAR or Technical Specifications. The Technical 
    Specifications required reviews of these tests and experiments are 
    not being proposed for removal by these requested amendments. Only 
    the organizational unit conducting the review of proposed tests and 
    experiments is being changed by the requested amendments. The PORC, 
    instead of the Station Manager, is being assigned the responsibility 
    for conducting the reviews of proposed tests and experiments in the 
    future. It is believed that the combined expertise of the PORC 
    membership will enhance Duke's ability to identify potential 
    situations which could possibly involve a new, or different, kind of 
    accident.
        Standard 3. The proposed amendments will not involve a 
    significant reduction in any margin of safety.
        The changes contained in the requested amendments are 
    administrative in nature and do not impact the design capabilities 
    or operation of any plant structures, systems, or components. There 
    will be no reduction in margin of safety as a result of implementing 
    these requested amendments. Impact upon margin of safety is a 
    consideration primarily included in the 10 CFR 50.59 evaluation 
    process conducted for station procedures, procedure changes, and 
    nuclear station modifications. The 10 CFR 50.59 evaluation process 
    is conducted under the auspices of the Duke Qualified Reviewer 
    Program and is not affected by these requested amendments. The 
    impact on margin of safety for future Technical Specifications and 
    Operating License changes will be reviewed by the PORC, but these 
    reviews will be equivalent in quality to the reviews presently 
    conducted by the Qualified Reviewers.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: January 27, 1995
        Description of amendment request: The requested change would modify 
    Section 5.3.1, Fuel Assemblies, of the Waterford 3 technical 
    specifications. The requested change increases the maximum enrichment 
    for the spent fuel pool and containment temporary storage rack from 4.1 
    to 4.9 weight percent U-235 when fuel assemblies contain fixed poisons. 
    Waterford 3 plans to use higher enriched fuel in the next fuel cycle 
    (Cycle 8) to meet the energy plans and maintain a reload batch size 
    similar to that used in Cycles 6 and 7.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change will increase the fuel enrichment limit in 
    order to meetthe cycle energy requirements while maintaining fuel 
    batch sizes consistent with previous cycle designs. The calculated 
    k-effective, including uncertainties, demonstrate substantial margin 
    to criticality in the storage racks for both normal and accident 
    conditions. No changes to the facility are required. No new modes of 
    operating the fuel storage or transfer systems are required, except 
    a restriction to limit the use of the new fuel vault to fuel with a 
    maximum enrichment of 4.1 weight percent U-235. This restriction 
    will be implemented by administrative controls. Since the plant 
    equipment and operation are essentially the same, there is no 
    significant increase in the probability of a criticality accident. 
    Since a criticality event is demonstrated to be unfeasible, there 
    are no increased adverse consequences for such a postulated event.
        As previously discussed, the proposed change will not result in 
    a physical change to the facility nor will it result in a 
    significant change to the operation of the facility; therefore, it 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed change has been analyzed to establish a k-
    effective, including uncertainties, at or below the NRC criticality 
    acceptance criteria of k-effective below 0.95 including 
    uncertainties at the 95/95 probability/confidence level; therefore, 
    there is no reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: January 16, 1995
        Description of amendment request: The proposed amendment would 
    revise the TMI-1 Technical Specifications (TS) to incorporate certain 
    improvements from the Revised Standard Technical Specifications (TS) 
    for Babcock & Wilcox nuclear power plants (NUREG-1430). The amendment 
    would also change the bases incorporating the results of analyses to 
    support allowance for drift of the pressurizer code safety valve 
    setpoint. One of the proposed STS improvements involves a change to 
    Chapter 6, Administrative Controls, affecting both TMI-1 and TMI-2 TSs. 
    A separate notice of consideration of issuance of amendment to facility 
    operating license is being issued for the proposed TMI-2 TSs Change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated.
        The proposed amendments involve a) an administrative change to 
    both the TMI-1 and TMI-2 Technical Specifications which is 
    consistent with the B&W Standard Technical Specifications (STS), 
    NUREG-1430, and b) changes to the TMI-1 Technical Specifications 
    which are consistent with the STS. This change does not involve any 
    change to system or equipment configuration. The proposed amendment 
    revises certain surveillance requirements, extends certain 
    surveillance intervals as evaluated above, or involves changes that 
    are purely
        administrative. The reliability of systems and components relied 
    upon to prevent or mitigate the consequences of accidents previously 
    evaluated is not degraded by the proposed changes. Assurance of 
    system and equipment availability is maintained. Therefore, this 
    change does not increase the probability of occurrence or the 
    consequences of an accident previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The changes 
    only involve changes to surveillance requirements that are 
    consistent with STS and with the ASME Code. No new failure modes are 
    created and thus the changes are bounded by accidents previously 
    evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not [[Page 14022]] involve a significant reduction 
    in a margin of safety. Each of these changes is compatible with the 
    STS and has been evaluated to preserve the level of safety assured 
    by the current TS.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Phillip F. McKee
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: January 20, 1995
        Description of amendment request: The proposed amendment would 
    revise the fire hazards analysis for the River Bend Station (RBS) by 
    allowing a deviation from 10 CFR 50, Appendix R, Section III.G.3 with 
    respect to the requirement for a fixed fire suppression system in fire 
    area C-17. This area houses the control building heating, ventilation 
    and air conditioning (HVAC) systems and the loss due to a fire could 
    cause the loss of main control room habitability. C-17 does not have a 
    fixed fire suppression system but depends upon the use of the existing 
    remote shutdown system as described in the updated safety analysis 
    report (USAR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) The request does not involve a significant increase in the 
    probability or consequences of accident previously evaluated.
        The event of concern is a fire in fire area C-17. The low fire 
    loading and sparse concentration of exposed combustible material in 
    fire area C-17 would limit fire spread. However, for this scenario 
    all equipment in fire area C-17 will be assumed lost. Fire area C-17 
    contains the air handling units for the main control room envelope. 
    The loss of both air handling units would cause the control building 
    chillers to stop running due to a logic tie requiring air flow 
    through the air handling equipment for the chilled water system to 
    operate during normal operation. The loss of the HVAC system in the 
    control building would cause the main control room and the equipment 
    rooms to begin heating up if exposed to design summer conditions. 
    Operator actions can be accomplished to minimize the heat up rates 
    for the rooms prior to the areas reaching equipment temperature 
    limits. This would allow the operators to begin the shutdown process 
    from the main control room. If the main control room continued to 
    heat up, the operators could accomplish the shutdown using the 
    remote shutdown system. HVAC for the remote shutdown panel is 
    located in fire area C-4 and would not be damaged by a fire in fire 
    area C-17. Operation of the control building HVAC system from the 
    remote shutdown panel bypasses the logic between the chilled water 
    system and the air handling system. This would allow restart of the 
    HVAC system for all areas except the main control room. The scenario 
    would conclude in a manner similar to that described in RBS USAR 
    Appendix 15A, Event 52, ``Reactor Shutdown From Outside Main Control 
    Room.''
        In summary, the probability of a fire occurring in fire area C-
    17 is not increased. However, if a fire were to occur in fire area 
    C-17 which caused the loss of main control room HVAC, the remote 
    shutdown system would provide an acceptable method of shutdown. The 
    low fire loading and sparse concentration of exposed combustible 
    material in fire area C-17 would limit fire spread. Therefore, this 
    request does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2) The request does not create the possibility of occurrence of 
    a new or different kind of accident from any accident previously 
    evaluated.
        The event of concern is a fire in fire area C-17. Fire area C-17 
    does not have a fixed suppression system as required by 10 CFR 50, 
    Appendix R, Section III.G.3. Fire suppression systems are generally 
    used to limit fire spread, once the heat of the fire opens thermally 
    sensitive sprinklers. The low fire loading and sparse concentration 
    of exposed combustible material in fire area C-17 would limit fire 
    spread. However, for the purpose of event analysis, all equipment in 
    fire area C-17 is assumed lost. Thus a fire in fire area C-17 is 
    bounded by the same analysis with or
        without a fixed suppression system in terms of equipment 
    availability.
        The proposed method of shutdown for a fire in fire area C-17 
    will be changed in that the remote shutdown system will be credited. 
    Use of the remote shutdown system is bounded by RBS USAR Appendix 
    15A, Event 52, ``Reactor Shutdown From Outside Main Control Room.'' 
    The HVAC for the remote shutdown panel is located in fire area C-4 
    and would be undamaged by a fire in fire area C-17. Operation of the 
    control building HVAC system from the remote shutdown panel bypasses 
    the logic between the chilled water system and the air handling 
    system. This would allow restart of the HVAC system for all areas 
    except the main control room.
        In summary, if a fire were to occur in fire area C-17 which 
    caused the loss of main control room HVAC, the remote shutdown 
    system would provide an acceptable method of shutdown. Since, for 
    the purpose of event analysis, all equipment in fire area C-17 is 
    assumed lost, a fire in fire area C-17 is bounded by the same 
    analysis with or without a fixed suppression system in terms of 
    equipment availability. Therefore, this request does not create the 
    possibility of occurrence of a new or different kind of accident 
    from any accident previously evaluated.
        3) The request does not involve a significant reduction in a 
    margin of safety.
        In this case, the margin of safety is implicit rather than being 
    explicitly expressed as a numerical value. An implicit margin of 
    safety involves conditions for NRC acceptance. Since the RBS 
    Technical Specification Bases do not specifically address a margin 
    of safety for fire protection, the SAR, the NRC's Safety Evaluation 
    Report (SER), and appropriate other licensing basis documents were 
    reviewed to determine if the proposed change would result in a 
    reduction in a margin of safety. As stated, in part, in Attachment 4 
    to NPF-47:
        EOI shall implement and maintain in effect all provisions of the 
    approved fire protection program as described in the Final Safety 
    Analysis Report for the facility through Amendment 22 and as 
    approved in the SER dated May 1984 and Supplement 3 dated August 
    1985 subject to provisions 2 and 3....
        As discussed in the Reason for Request, SSER 3 dated August 1985 
    states, in part:
        On the basis of its evaluation the staff finds that the 
    applicant's fire protection program with approved deviations is in 
    conformance with the guidelines of BTP CMEB 9.5-1, sections III.G, 
    III.J, and III.O of Appendix R to 10CFR50, and GDC 3, and is, 
    therefore, acceptable.
        Thus, the margin of safety in this case can be defined as 
    conformance with the specified fire protection guidelines. 10 CFR 
    50, Appendix R, Section III.G.3, requires, in part, that alternative 
    shutdown capability be provided for areas where adequate separation 
    of redundant safe shutdown components cannot be provided. In 
    addition, fire detection and a fixed fire suppression system must be 
    installed in the area, room, or zone under consideration. Since fire 
    area C-17 does not have a fixed suppression system, use of the 
    remote shutdown system for a fire in this fire area would deviate 
    from the requirements of 10 CFR 50, Appendix R, Section III.G.3. 
    However, as discussed previously, the low fire loading and sparse 
    amount of exposed combustibles compensate for the lack of a fixed 
    fire suppression system. There is no adverse impact on the ability 
    to achieve and maintain safe shutdown. Therefore, this request does 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    [[Page 14023]] amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Northeast Nuclear Energy Company (NNECO), Docket No. 50-245, 
    Millstone Nuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of amendment request: July 28, 1994
        Description of amendment request: The proposed amendment would add 
    a footnote to Technical Specifcaiton 3.5.C. The footnote would state 
    that the operability of the feedwater coolant injection (FWCI) system 
    be independent of its seismic capability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed change in accordance with 
    10CFR50.92 and concluded that the change does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    compromised. The proposed change does not involve an SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        Any postulated failure in the non-seismic portion of the FWCI 
    subsystem may result in a loss of feedwater flow transient. However 
    comparing the probability of occurrence of a seismic event, any 
    increase in the probability of occurrence of a loss of feedwater 
    event would be small. The proposed change would have no impact on 
    the probability of occurrence of any other accident, including LOCAs 
    [loss of coolant accidents].
        The FWCI subsystem will continue to be maintained as QA Category 
    1 (except for the seismic attribute). Therefore, it will remain 
    available for accident mitigation for most scenarios. Nevertheless, 
    LOCA analyses have been reevaluated to demonstrate that FWCI is not 
    necessary to show compliance with 10CFR50.46. Potentially limiting 
    LOCA scenarios have been analyzed without the FWCI subsystem using 
    an approved LOCA methodology. An active single failure was 
    postulated in addition to not taking credit for the FWCI subsystem. 
    Based on the results of these analyses, the current design basis 
    large and small break LOCAs remain bounding. Moreover, FWCI is not 
    credited in mitigating any of the non-LOCA transients/accidents.
        Safe shutdown following a seismic event can be achieved using 
    the LPCI [low pressure coolant injection] and ESW [emergency service 
    water] systems, and the SRVs [safety relief valves], which are all 
    seismically qualified. Therefore, the FWCI system is not required to 
    mitigate a seismic event.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        Seismic reclassification of portions of FWCI does not create the 
    possibility of a new kind of an accident. The portion of the piping 
    up to the second isolation valve (from the RPV [reactor pressure 
    vessel]), is seismically qualified and will remain classified as 
    seismic. This ensures that a postulated failure in the non-seismic 
    portion of piping or components does not degrade containment 
    integrity or result in a blowdown of the RPV. Consequential and 
    environmental effects of a FW [feedwater] piping failure have been 
    analyzed in the HELB [high energy line break] program and have been 
    found to be acceptable.
        3. Involve a significant reduction in the margin of safety.
        All accidents, including LOCAs, can be mitigated without using 
    FWCI. FWCI is also not necessary for safe shutdown following a 
    seismic event. The intended function of the FWCI subsystem is to 
    reduce the likelihood of core uncovery during the lifetime of the 
    plant. The CS [core spray] and LPCI subsystems provide redundant and 
    diverse means of injecting water to the RPV. The FWCI subsystem 
    provides an additional diverse means to inject water. Since FWCI 
    will be maintained QA Category 1 (except for the seismic attribute), 
    it will continue to provide the additional diversity to the 
    injection systems. Considering the intended function of the 
    subsystem and the credit taken in the accident analysis, 
    reclassifying FWCI to be non-seismic does not significantly reduce 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: January 9, 1995, as supplemented 
    February 7, 1995
        Description of amendment requests: The proposed amendments would 
    revise Prairie Island Nuclear Generating Plant Technical Specification 
    (TS) 4.12, ``Steam Generator Tube Surveillance,'' to incorporate 
    revised acceptance criteria for steam generator tubes with degradation 
    in the tubesheet roll expansion region. These criteria for steam 
    generator tube acceptance were developed by Westinghouse Electric 
    Corporation and are known as F* (F-Star'') and L* 
    (L-Star''). These criteria would be utilized to avoid 
    unnecessary plugging and sleeving of steam generator tubes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        F* Steam Generator Tube Repair Criteria
        The supporting technical and safety evaluations of the subject 
    criterion demonstrate that the presence of the tubesheet will 
    enhance the tube integrity in the region of the hardroll by 
    precluding tube deformation beyond its initial expanded outside 
    diameter. The resistance to both tube rupture and tube collapse is 
    strengthened by the presence of the tubesheet in that region. The 
    results of hardrolling of the tube into the tubesheet is an 
    interference fit between the tube and the tubesheet. Tube rupture 
    cannot occur because the contact between the tube and tubesheet does 
    not permit sufficient movement of tube material. The radial preload 
    developed by the rolling process will secure a postulated separated 
    tube end within the tubesheet during all plant conditions. In a 
    similar manner, the tubesheet does not permit sufficient movement of 
    tube material to permit buckling collapse of the tube during 
    postulated LOCA [loss-of-coolant accident] loadings.
        The F* length of roll expansion is sufficient to preclude tube 
    pullout from tube degradation located below the F* distance, 
    regardless of the extent of the tube degradation. The existing 
    Technical Specification leakage rate requirements and accident 
    analysis assumptions remain unchanged in the unlikely event that 
    significant leakage from this region does occur. As noted above, 
    tube rupture and pullout is not expected for tubes using the F* 
    criterion. Any leakage out of the tube from [[Page 14024]] within 
    the tubesheet at any elevation in the tubesheet is fully bounded by 
    the existing steam generator tube rupture analysis included in the 
    Prairie Island Plant USAR [Updated Safety Analysis Report]. For 
    plants with partial depth roll expansion like Prairie Island, a 
    postulated tube separation within the tube near the top of the roll 
    expansion (with subsequent limited tube axial displacement) would 
    not be expected to result in coolant release rates equal to those 
    assumed in the USAR for a steam generator tube rupture event due to 
    the limited gap between the tube and tubesheet. The proposed 
    plugging criterion does not adversely impact any other previously 
    evaluated design basis accident.
        Leakage testing of roll expanded tubes indicates that for roll 
    lengths approximately equal to the F* distance, any postulated 
    faulted condition primary to secondary leakage from F* tubes would 
    be insignificant.
        L* Steam Generator Tube Repair Criteria
        The presence of the tubesheet enhances steam generator tube 
    integrity in the region of the hardroll by precluding tube 
    deformation beyond its initial expanded outside diameter. The 
    resistance to both tube rupture and tube collapse is strengthened by 
    the presence of the tubesheet in that region. The result of the 
    hardroll of the tube into the tubesheet is an interference fit 
    between the tube and the tubesheet. Tube rupture cannot occur 
    because the contact between the tube and tubesheet does not permit 
    sufficient movement of tube materials. In a similar manner, the 
    tubesheet does not permit sufficient movement of tube material to 
    permit buckling collapse of the tube during postulated LOCA 
    loadings.
        The type of degradation for which the L* criteria has been 
    developed (cracking with an axial or near axial orientation) has 
    been found not to significantly reduce the axial strength of a tube. 
    An evaluation including analysis and testing has been done to 
    determine the strength reduction for the axial loads with simulated 
    axial and near axial cracks. This evaluation provided the basis for 
    the acceptance criteria for tube degradation subject to the L* 
    criteria.
        The length of roll expansion above L* is sufficient to preclude 
    significant leakage from tube degradation located below the L* 
    distance. The existing Technical Specification leakage rate 
    requirements and accident analysis assumptions remain unchanged in 
    the unlikely event that significant leakage from this region does 
    occur. As noted above, tube rupture and pullout is not expected for 
    tubes using the alternate plugging criteria.
        Any leakage out of the tube from within the tubesheet at any 
    elevation in the tubesheet is fully bounded by the existing steam 
    generator tube rupture analysis included in the Prairie Island 
    Updated Safety Analysis Report. The proposed alternate plugging 
    criteria do not adversely impact any other previously evaluated 
    design basis accident.
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        F*
        Implementation of the proposed F* criterion does not introduce 
    any significant changes to the plant design basis. Use of the 
    criterion does not provide a mechanism to initiate an accident 
    outside of the region of the expanded portion of the tube. Any 
    hypothetical accident as a result of any tube degradation in the 
    expanded portion of the tube would be bounded by the existing tube 
    rupture accident analysis. Tube bundle structural integrity will be 
    maintained. Tube bundle leaktightness will be maintained such that 
    any postulated accident leakage from F* tubes will be negligible 
    with regards to offsite doses.
        L*
        Implementation of the proposed alternate tubesheet tube plugging 
    criteria does not introduce changes to the plant design basis. Use 
    of the criteria does not provide a mechanism to result in an 
    accident outside of the region of the tubesheet expansion. Any 
    hypothetical accident as a result of any tube degradation in the 
    expanded portion of the tube would be bounded by the existing tube 
    rupture accident analysis.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety.
        F*
        The use of the F* criterion has been demonstrated to maintain 
    the integrity of the tube bundle commensurate with the requirements 
    of Reg Guide 1.121 [Bases for Plugging Degraded PWR Steam 
    Generator Tubes] (intended for indications in the free 
    span of tubes) and the primary to secondary pressure boundary under 
    normal and postulated accident conditions. Acceptable tube 
    degradation for the F* criterion is any degradation indication in 
    the tubesheet region, more than the F* distance below the bottom of 
    the transition between the roll expansion and the unexpanded tube. 
    The safety factors used in the verification of the strength of the 
    degraded tube are consistent with the safety factors in the ASME 
    Boiler and Pressure Vessel Code used in steam generator design. The 
    F* distance has been verified by testing to be greater than the 
    length of roll expansion required to preclude both tube pullout and 
    significant leakage during normal and postulated accident 
    conditions. Resistance to tube pullout is based upon the primary to 
    secondary pressure differential as it acts on the surface area of 
    the tube, which includes the tube wall cross-section, in addition to 
    the inner diameter based area of the tube. The leak testing 
    acceptance criteria are based on the primary to secondary leakage 
    limit in the Technical Specifications and the leakage assumptions 
    used in the USAR accident analysis.
        Implementation of the tubesheet plugging criterion will decrease 
    the number of tubes which must be taken out of service with tube 
    plugs or repaired with sleeves. Both plugs and sleeves reduce the 
    RCS (reactor coolant system) flow margin; thus, implementation of 
    the F* criterion will maintain the margin of flow that would 
    otherwise be reduced in the event of increased plugging or sleeving.
        Based on the above, it is concluded that the proposed change 
    does not result in a significant reduction in margin with respect to 
    plant safety as defined in the USAR or the Technical Specification 
    Bases.
        L*
        The use of the alternate tubesheet plugging criteria has been 
    demonstrated to maintain the integrity of the tube bundle 
    commensurate with the requirements of Reg. Guide 1.121 for 
    indications in the free span of tubes and the primary to secondary 
    pressure boundary under normal and postulated accident conditions. 
    Acceptable tube degradation for the L* criteria is any degradation 
    indication with axial or nearly axial cracking in the tubesheet 
    region, more than the L* distance below the bottom of the transition 
    between the roll expansion and the unexpended tube. For tubes with 
    axial or nearly axial cracks the strength of the tube relative to an 
    axial load would not be reduced below the strength required to 
    resist potential axial loads. The safety factors used in the 
    verification of the strength of the degraded tube are consistent 
    with the safety factors in the ASME Boiler and Pressure Vessel Code 
    used in steam generator design. The L* distance has been verified by 
    testing to be greater than the length of roll expansion required to 
    preclude significant leakage during normal and postulated accident 
    conditions. The leak testing acceptance criteria are based on the 
    primary to secondary leakage limit in the Technical Specifications 
    and the leakage assumptions used in the USAR accident analyses.
        Implementation of the proposed tubesheet plugging criteria will 
    decrease the number of tubes which must be taken out of service with 
    tube plugs or repaired with sleeves. Both plugs and sleeves reduce 
    the RCS flow margin, thus implementation of the alternate plugging 
    criteria will maintain the margin of flow that would otherwise be 
    reduced in the event of increased plugging or sleeving.
        Based on the above, it is concluded that the proposed change 
    does not result in a significant reduction in margin with respect to 
    plant safety as defined in the Updated Safety Analysis Report or the 
    bases of the Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration. This 
    notice supersedes the staff's previous notice which was published in 
    the Federal Register February 1, 1995 (60 FR 6307).
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Cynthia Carpenter, Acting [[Page 14025]] 
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: February 23, 1995
        Description of amendment requests: The proposed amendments would 
    revise the wording in the Prairie Island technical specifications to 
    allow implementation of exemptions to the schedule requirements of 10 
    CFR Part 50, Appendix J. A related exemption request would grant 
    temporary relief from the requirements of 10 CFR Part 50, Appendix J, 
    Section III.D.1.(a) which requires Prairie Island Unit 2 to perform a 
    Type A test in the May 1995 refueling outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment is an administrative change which allows 
    implementation of approved exemptions to the regulations and by 
    itself does not change any retest schedules.
        Therefore, the probability or consequences of an accident 
    previously evaluated are not affected by the proposed amendment.
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        The proposed amendment is an administrative change which allows 
    implementation of approved exemptions to the regulations and by 
    itself does not change any retest schedules.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be created 
    by the proposed amendment.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety
        The proposed amendment is an administrative change which allows 
    implementation of approved exemptions to the regulations and by 
    itself does not change any retest schedules.
        Therefore, a significant reduction in the margin of safety would 
    not be involved with the proposed amendment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Cynthia Carpenter, Acting
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station,Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: February 10, 1995
        Description of amendment request: The proposed amendment to the 
    technical specifications (TSs) would relocate the requirements for the 
    incore instrumentation (ICI) system from the TS to the Updated Safety 
    Analysis Report (USAR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Incore Instrumentation (ICI) System is used to measure core 
    power distribution for the purpose of Limiting Conditions for 
    Operation (LCO) monitoring of Technical Specification (TS) limits on 
    linear heat rate, unrodded planer radial peaking factor, unrodded 
    integrated radial peaking factor, and azimuthal power tilt. The ICI 
    System has no safety purpose itself; it measures parameters which 
    have safety significance. No change to the monitored parameters is 
    proposed. The proposed changes will relocate requirements on the 
    number and distribution of incore detectors used by the ICI System 
    when measuring these parameters from the TS to the Updated Safety 
    Analysis Report (USAR). Changes to the requirements can be made 
    without NRC approval when the changes meet the criteria of 10 CFR 
    50.59. Changes to the ICI System requirements that do not meet the 
    criteria of 10 CFR 50.59 must be approved by the NRC by license 
    amendment.
        Relocation of the requirements on the ICI System from the TS to 
    the USAR does not increase the probability or consequences of any 
    accident previously analyzed because the ICI System is neither a 
    precursor nor a mitigator for any analyzed accident. The ICI System 
    is used to ensure that operation within the LCOs for linear heat 
    rate, unrodded planer radial peaking factor, unrodded integrated 
    radial peaking factor, and azimuthal power tilt is maintained. 
    However, its operation serves no mitigation function associated with 
    any USAR Section 14 accident analysis. The parameters measured by 
    the ICI System are important parameters in many accident analyses; 
    however, this proposed change does not remove or revise the limits 
    on these parameters.
        Additionally, it is proposed to revise TS 2.10.4(1)(b) to 
    clarify its requirements. Currently TS 2.10.4(1) part (b) applies 
    while operating under the provisions of part (a) if the plant 
    computer incore detector alarms become inoperable. This is incorrect 
    in that part (a) applies when the linear heat rate is being 
    monitored by the ICI System and the linear heat rate is exceeding 
    its limits as indicated by valid detector alarms. Part (b) of this 
    specification should apply only if the linear heat rate is being 
    monitored by the ICI System, is within its limits, and the plant 
    computer incore detector alarms are inoperable.
        Administrative changes are also proposed which correct grammar 
    and renumber/relocate portions of the TS and bases to other TS, to 
    correspond to the proposed change to relocate ICI System 
    requirements.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        (2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The ICI System will continue to be used to monitor TS limits on 
    core power distribution. There will be no physical alterations to 
    the plant configuration, changes to setpoint values, or changes to 
    the implementation of setpoints or limits as a result of this 
    proposed change.
        The proposed change to TS 2.10.4(1)(b) only clarifies its 
    requirements. The proposed change is more restrictive in that TS 
    2.10.4(1)(b), as currently written, could be interpreted to allow 
    continued operation for up to seven days with the linear heat rate 
    exceeding its limits. The proposed change clarifies this 
    specification to ensure that TS 2.10.4(1)(a) is applied if the 
    linear heat rate is exceeded while being monitored by the ICI 
    System. TS 2.10.4(1)(a) requires that the linear heat rate be 
    restored within one hour or a plant shutdown initiated.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        (3) The proposed changes do not involve a significant reduction 
    in a
        margin of safety.
        The ICI System is used to measure core power distribution 
    parameters which are a direct measure of the margin of safety. The 
    limits on these parameters are not changed. Therefore, the proposed 
    change (i.e., relocation of the ICI System operability requirements 
    to the USAR and/or plant procedures) does not involve a significant 
    reduction in a margin of safety.
        The proposed change to TS 2.10.4(1)(b) helps ensure that the 
    margin of safety is maintained by clarifying when the TS is 
    applicable. This clarification ensures that the more restrictive 
    actions of TS 2.10.4(1)(a) are taken if the linear heat rate is 
    exceeded while being monitored by the ICI System. Therefore, the 
    proposed change does not involve a significant reduction in a margin 
    of safety. [[Page 14026]] 
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: LeBoeuf, Lamb, Leiby, and MacRae, 1875 
    Connecticut Avenue, NW., Washington, DC 20009-5728
        NRC Project Director: Theodore R. Quay
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    DiabloCanyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: December 30, 1994 (Reference LAR 94-12)
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Nuclear Power Plant, Unit Nos. 1 and 2, to revise TS 2.2, 3/4.3.1, 3/
    4.3.2, 3/4.3.3, 3/4.4.4, 3/4.4.9, 3/4.5.2, 3/4.8.1, 3/4.8.2, 3/4.9.2, 
    3/4.9.9, and 3/4.10.3. The specific TS changes proposed are as follows:
        (1) The TS issued in License Amendments (LAs) 84/83 would be 
    changed to (a) revise the value of the overpower Delta-temperature 
    (OPDT) constant K6 in TS 2.2.1, Table 2.2-1, Note 3; (b) revise the 
    reactor coolant system (RCS) loop Delta-T function; and (c) make 
    editorial corrections for clarification and consistency to TS 2.2.1 
    (and TS 2.2.1 Bases), TS 3/4.3.1, and TS 3/4.3.2.
        In revising the RCS loop Delta-T function, the licensee would (a) 
    incorporate the 0.99 multiplying factor listed in TS 2.2.1, Table 2.2-
    1, Note 5, and TS 3/4.3.2, Table 3.3-4, Note 2, into constants B1 
    through B4; (b) change ``Steam Generator (SG) Water Level Low-Low'' in 
    TS 3/4.3.2, Table 3.3-3 and Table 4.3-2, Functional Unit 6.c, 
    ``Auxiliary Feedwater'' (AFW), by deleting the Mode 3 applicability of 
    the RCS loop Delta-T function and by adding a footnote to the Mode 3 
    applicability of the SG water level low-low function requiring that the 
    trip time delay (TTD) associated with the SG water level low-low 
    channel be less than or equal to 464.1 seconds; (c) change TS 3/4.3.1, 
    Table 3.3-1, Action 27, and TS 3/4.3.2, Table 3.3-3, Action 29, by 
    allowing up to four RCS loop Delta-T channels to be inoperable with the 
    TTD threshold power level for zero seconds time adjusted to 0-percent 
    rated thermal power (RTP) and by allowing the affected SG water level 
    low-low channels to be placed in the tripped condition, with one 
    inoperable RCS loop Delta-T channel; and (d) change the Table 3.3-1 and 
    Table 3.3-3 ``Channels to Trip'' and ``Minimum Channels Operable'' 
    columns to not applicable (N.A.).
        (2) The TS issued in LAs 70/69 would be changed to (a) delete 
    references to the plant vent noble gas activity monitors (RM-14A and 
    RM-14B) and footnote references to applicability of the containment 
    ventilation exhaust radiation monitors (RM-44A and RM-44B) in TS Tables 
    3.3-3, 3.3-4, 3.3-5, 3.3-6, 4.3-2, and 4.3-3 and TS 4.9.9; and (b) 
    revise the ``Trip Setpoint and Allowable Values'' column in TS Table 
    3.3-4, Functional Unit 3.c.4), to reference the offsite dose 
    calculation procedure (ODCP).
        (3) Cycle-specific information in TS 4.3.2.1, TS 3.3.3.6, TS 
    4.4.4.1, TS 4.5.2, TS 3.8.1.1, TS 3.8.2.1, and TS 3.8.2.2 that is no 
    longer necessary would be deleted.
        (4) The word ``analog'' would be deleted from TS 4.4.9.3.1, TS 
    4.9.2, and TS 4.10.3.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change to the OPDT constant K6 is conservative and 
    will not cause any design or analysis acceptance criteria to be 
    exceeded. There is no effect on the structural and functional 
    integrity of any plant system. The OPDT function is part of the 
    accident mitigation response and is not itself an initiator for any 
    transient. This change does not affect the integrity of the fission 
    product barriers for mitigation of radiological dose consequences as 
    a result of an accident.
        The proposed change to incorporate the 0.99 multiplier into the 
    TTD constants is an administrative change and has no effect on plant 
    operation. The proposed change to delete Mode 3 applicability of the 
    RCS Loop Delta-T function does not affect any design or analysis 
    results. Allowing up to 4 RCS Loop Delta-T channels to be inoperable 
    with the TTD threshold power level for zero seconds time delay 
    adjusted to 0% RTP is conservative with respect to ESFs [engineered 
    safety features] and reactor trip actuation time. Allowing the SG 
    [steam generator] water level low-low channels affected by the 
    inoperable RCS Loop Delta-T channels to be placed in the tripped 
    condition is also conservative with respect to reactor trip and AFW 
    pumps start. The change to the Channels to Trip and Minimum Channels 
    Operable columns is a clarifying change to reflect the proposed 
    changes to the action statements and identifies that the RCS Loop 
    Delta-T does not provide a reactor trip function. Therefore, the 
    proposed changes to the RCS Loop Delta-T function do not affect any 
    of the accident analysis results.
        The proposed changes to revise Table 3.3-4, Functional Unit 
    3.c.4), and to delete cycle-specific TS, TS references to RM-14A and 
    RM-14B, and the word ``analog'' from the analog channel operation 
    test are administrative and have no effect on plant operation.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change to the OPDT constant K6 does not affect the 
    assumed accident initiation sequences. No new operating 
    configuration is being imposed by the change to K6 that would create 
    a new failure scenario. No new failure modes are being created for 
    any plant equipment.
        The proposed changes to the RCS Loop Delta-T function do not 
    involve any physical modification to any plant system or change the 
    methodology by which any safety-related system performs its 
    function.
        1The proposed changes to revise Table 3.3-4, Functional Unit 
    3.c.4), and to delete cycle-specific TS, TS references to RM-14A and 
    RM-14B, and the word ``analog'' from the analog channel operation 
    test are administrative, would not result in any physical alteration 
    to any plant system, and would not be a change in the method by 
    which any safety-related system performs its function.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed change to the OPDT constant K6 will not affect any 
    accident analysis assumptions, initial conditions, or results.
        The proposed changes to the RCS Loop Delta-T function do not 
    affect any accident analysis assumptions, initial conditions, or 
    results.
        The proposed changes to revise Table 3.3-4, Functional Unit 
    3.c.4), and to delete cycle-specific TS, TS references to RM-14A and 
    RM-14B, and the word ``analog'' from the analog channel operation 
    test are administrative and clarify the TS. These proposed changes 
    have no effect on current operating methodologies or actions that 
    govern plant performance.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests [[Page 14027]] involve no significant hazards 
    consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Theodore R. Quay
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company,Delmarva Power and Light Company, and Atlantic City 
    Electric Company,Dockets Nos. 50-277 and 50-278, Peach Bottom 
    Atomic Power Station,Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: September 26, 1994
        Description of amendment request: The proposed TS changes extend 
    surveillance test intervals and allowable out-of-service times for the 
    testing and/or repair of instrumentation that actuate the Reactor 
    Protection System, Primary Containment Isolation, Core and Containment 
    Cooling systems, Control Rod Blocks, Radiation Monitoring systems, and 
    Alternate Rod Insertion/Recirculation Pump Trip.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed TS changes increase the STIs and AOTs for actuation 
    instrumentation based on analyses described and justified in 
    Licensing Topical Reports (References 2 through 8) [see licensee's 
    September 26, 1994 application for reference information] which have 
    been evaluated in associated Safety Evaluation Reports. These 
    changes were incorporated into PBAPS Technical Specifications 
    consistent with NUREG-1433. TS requirements that govern Operability 
    or routine testing of plant instruments are not assumed to be 
    initiators of any analyzed event because these instruments are 
    intended to prevent, detect or mitigate accidents. Therefore, these 
    changes will not involve an increase in the probability of 
    occurrence of an accident previously evaluated. Additionally, these 
    changes will not increase the consequences of an accident previously 
    evaluated because the proposed change will not involve any physical 
    changes to plant systems, structures, or components (SSC), or the 
    manner in which these SSC are operated, maintained, modified, or 
    inspected. The changes will not alter the operation of equipment 
    assumed to be available for the mitigation of accidents or 
    transients by the plant safety analysis or licensing basis. As 
    justified in References 1 through 8, the proposed changes establish 
    or maintain adequate assurance that components are operable when 
    necessary for the prevention or mitigation of accidents or 
    transients and that plant variables are maintained within limits 
    necessary to satisfy the assumptions for initial conditions in the 
    safety analyses. These changes establish or modify time limits 
    allowed for operation with inoperable instrument channels based on 
    the analyses in References 1 through 8 and will not allow continuous 
    plant operation with plant conditions such that a single failure 
    will result in a loss of any safety function. Therefore, these 
    changes will not increase the consequences of an accident previously 
    evaluated.
        2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        These proposed changes will not involve any physical changes to 
    SSC, or the manner in which these SSC are operated, maintained, 
    modified, tested, or inspected. Therefore, these changes will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated. The changes in methods governing 
    normal plant operation are consistent with the current safety 
    analysis assumptions. Therefore, these changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3) The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed TS changes increase the STIs and AOTs for actuation 
    instrumentation based on analyses described and justified in 
    Licensing Topical Reports (References 2 through 8) which have been 
    evaluated in associated Safety Evaluation Reports. These changes 
    were incorporated into PBAPS Technical Specifications consistent 
    with NUREG-1433. These changes can be classified into one of the 
    following three categories:
        a. Changes to the minimum STIs and AOTs for the testing and/or 
    repair of instrumentation based on the results of generic analyses 
    in References 1 through 8;
        b. Changes to conditions, required actions, and completion times 
    needed to make PBAPS TS requirements consistent with the assumptions 
    used in the analyses in References 1 through 8; and,
        c. Changes that reformat, renumber, and/or reword existing 
    requirements to incorporate the changes above.
        All of the proposed changes will be incorporated into the PBAPS 
    custom Technical Specifications using the same approach and specific 
    requirements used in Reference 12.
        There is no significant reduction in the margin of safety 
    resulting from changes to the STIs and AOTs for the testing and/or 
    repair of instrumentation based on the results of the analyses in 
    References 1 through 8. These analyses determined that there is no 
    significant change in the availability and/or reliability of 
    instrumentation as a result of this change in STIs and AOTs. PECO 
    Energy performed reviews that confirmed these analyses are 
    applicable to PBAPS and that there would be no effect on the 
    identification of excessive instrument setpoint drift as a result of 
    increasing from monthly to quarterly the minimum interval between 
    instrument functional tests. The proposed required actions ensure 
    that actions to mitigate loss of single failure tolerance is 
    initiated within 24 hours (12 hours for RPS) in accordance with the 
    results of the analyses in References 1 through 8 and action to 
    mitigate a loss of instrument function is initiated within 1 hour.
        The proposed changes which replace the shutdown actions 
    associated with inoperable instrumentation with actions to declare 
    the supported system inoperable does not involve a reduction in a 
    margin of safety. The proposed changes ensure that appropriate 
    compensatory measures are taken commensurate with approved TS 
    Actions for the affected systems and the safety analyses. In 
    addition, the proposed changes provide the benefit of avoiding an 
    unnecessary shutdown transient when appropriate measures are 
    available to compensate for the inoperable instrumentation.
        There is no significant reduction in the margin of safety 
    resulting from changes that reformat, renumber, and/or reword 
    existing requirements to incorporate the changes above.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: John F. Stolz
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company,Delmarva Power and Light Company, and Atlantic City 
    Electric Company,Dockets Nos. 50-277 and 50-278, Peach Bottom 
    Atomic Power Station,Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 17, 1994
        Description of amendment request: The proposed changes to the 
    Technical Specifications (TS) are being requested to support 
    modifications 5384 and 5386 which upgrade the Main Stack and Vent Stack 
    Radiation Monitoring Systems. [[Page 14028]] 
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Neither the Main Stack nor the Vent Stack Radiation Monitoring 
    Systems serve as an initiator or contributor to any accidents 
    previously evaluated. The systems provide indication and detection 
    of radioactivity and effluent release in the main and vent stacks. 
    The new systems perform the same function as the old, and have equal 
    or better performance characteristics. Installation and operation of 
    the new radiation monitoring systems do not degrade any active or 
    passive equipment that responds to an accident.
        The proposed increase in the surveillance test interval of the 
    subject radiation monitoring systems from 12 to 18 months is 
    consistent with vendor recommendations, and is based on operating 
    experience with instrumentation of a similar design.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Both modifications replace obsolete radiation monitoring 
    equipment and have the same failure modes as the existing equipment. 
    The upgraded systems are considered enhancements to the existing 
    systems and are considered neither a contributor nor initiator of 
    any accidents previously evaluated.
        Based on the above, the proposed changes do not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        Neither the accuracy nor the responsiveness of the existing 
    radiation monitoring equipment will be degraded as a result of the 
    installation of modifications 5384 and 5386. Revisions to the 
    calibration and surveillance frequencies are based on vendor 
    information and experience with instrumentation of similar design. 
    The changes associated with setpoints and the lower limit of 
    detection are in the conservative direction. The upgraded main stack 
    system continues to provide a non-safety related trip signal to 
    Group III isolation valves during purging of the containment through 
    the SBGTS [standby gas treatment system]. The revisions to parameter 
    descriptions and instrument designation are considered 
    administrative.
        Therefore, based on the above, the proposed changes do not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket No. 50-311, Salem 
    Nuclear Generating Station, Unit No. 2, Salem County, New Jersey
    
        Date of amendment request: February 3, 1994, supplemented September 
    19, 1994, and November 23, 1994
        Description of amendment request: The proposed amendment revises 
    the Technical Specifications to reflect a reduction in the Reactor 
    Coolant System flow.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        No component modification, system realignment, or change in 
    operations will occur which could affect the probability of any 
    accident or transient. The proposed reduction in RCS loop and total 
    flow rates will not change the probability of a challenge to any 
    Engineered Safeguard Feature or other device. The consequences of 
    previously analyzed accidents have been found to remain within 
    acceptable licensing basis limits when the reduced flow rates are 
    assumed. The system transient response is not affected by the 
    initial RCS flow assumption, unless the initial assumption is so low 
    as to impair the steady-state core cooling capability or steam 
    generator heat transfer capability. This is clearly not the case 
    with a 1% reduction in RCS flow. The proposed change to the wording 
    of the parameter title on Table 3.2-1 is editorial for clarity. 
    Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        2. Create the possibility of a new or different kind of 
    accident.
        No component modification, system realignment, or change in 
    operating procedure will occur which could create the possibility of 
    a new event not previously considered. The proposed reduction in RCS 
    loop and total flow rates will not initiate any new events. 
    Therefore, the proposed changes would not create the possibility of 
    a different or new kind of accident.
        3. Involve a significant reduction in a margin of safety.
        The proposed decrease in RCS loop and total flow rates has been 
    analyzed and found to have an insignificant effect on the applicable 
    transient analyses found in the FSAR. The proposed change to the 
    wording of the parameter title on Table 3.2-1 is editorial for 
    clarity. Therefore, the proposed changes would not involve a 
    significant reduction in any margin of safety.
        Therefore, based on the information presented above, PSE&G has 
    concluded there is no significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: January 30, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 4.6.1.2.a and associated Bases for 
    3/4.6.1.2 to state that Type A tests for overall integrated containment 
    leakage rate shall be conducted in accordance with the requirements 
    specified in Appendix J of 10 CFR 50, as modified by NRC-approved 
    exemptions. Additionally, TS 4.6.1.2.b would be revised to eliminate 
    the reference to the schedule contained in TS 4.6.1.2.a.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Toledo Edison has reviewed the proposed change and determined 
    that a significant hazards consideration does not exist because 
    operation of the Davis-Besse Nuclear Power Station, Unit No. 1, in 
    accordance with these changes would:
        1a. Not involve a significant increase in the probability of an 
    accident previously evaluated because no accident initiators, 
    [[Page 14029]] 
        conditions or assumptions are significantly affected by the 
    proposed changes.
        The proposed change would revise Technical Specification (TS) 
    Surveillance Requirement (SR) 4.6.1.2.a to allow overall integrated 
    containment leakage rate (Type A) testing to be scheduled in 
    accordance with 10 CFR 50 Appendix J, as modified by approved 
    exemptions, and would make associated administrative changes to TS 
    SR 4.6.1.2.b and to TS Bases 3/4.6.1.2. As stated above, none of 
    these proposed changes involve accident initiators, conditions, or 
    assumptions.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because no accident conditions or 
    assumptions are affected by the proposed changes.
        The results of the previous Type A testing demonstrate a high 
    degree of containment integrity. The Type B and C testing performed 
    since the last Type A test provides confidence that the high degree 
    of containment integrity will be maintained during the interval to 
    the next Type A test. Therefore, the proposed changes do not alter 
    the source term, containment isolation, or allowable releases, and 
    will not increase the radiological consequences of a previously 
    evaluated accident.
        2. Not create the possibility of a new or different kind of 
    accident from any accident previously evaluated because no new or 
    different accident initiators or assumptions are introduced by the 
    proposed changes. The proposed changes do not affect the design or 
    operation of any plant system, structure, or component. The proposed 
    changes do not affect any accident initiators and are not initiators 
    themselves. The proposed changes do not alter any accident 
    scenarios.
        3. Not involve a significant reduction in a margin of safety. 
    The initial conditions and methodologies used in the accident 
    analyses remain unchanged. As described above, the proposed changes 
    do not significantly reduce or adversely affect the confidence that 
    the present high degree of containment integrity will be maintained.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: January 30, 1995
        Description of amendment request: The proposed amendment would 
    provide new Reactor Coolant Pressure Boundary (RCPB) pressure-
    temperature limit curves that are applicable up to 21 effective full 
    power years (EFPY).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Toledo Edison had reviewed the proposed change and determined 
    that a significant hazards consideration does not exist because 
    operation of Davis-Besse Nuclear Power Station, Unit 1, in 
    accordance with this change would:
        1a. Not involve a significant increase in the probability of an 
    accident previously evaluated because: (1) revision of the pressure-
    temperature curves and the extended applicability of the pressurizer 
    level/RCS pressure limit curves for periods when relief valve DH4849 
    is inoperable will continue to provide the same level of protection 
    of the RCPB as was previously evaluated, and (2) the revision to 
    License Condition 2.C(3)(d) is administrative to reflect the 
    validity of the present analyses to 21 EFPY and (3) the revision to 
    the Technical Specification Bases
        to reflect the extension to 21 EFPY is administrative and does 
    not affect any previously analyzed accidents.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because: (1) revision of the pressure-
    temperature curves and the extended applicability of the pressurizer 
    level/RCS pressure limit curves for periods when relief valve DH4849 
    is inoperable will continue to provide the same level of protection 
    of the RCPB as was previously evaluated, and (2) the revision to 
    License Condition 2.C(3)(d) is administrative to reflect the 
    validity of the present analyses to 21 EFPY and (3) the revision to 
    the Technical Specification Bases to reflect the extension to 21 
    EFPY is administrative and does not affect any previously analyzed 
    accidents.
        2. Not create the possibility of a new or different kind of 
    accident from any accident previously evaluated because: (1) 
    revision of the pressure-temperature curves and the extended 
    applicability of the pressurizer level/RCS pressure limit curves 
    will continue to provide protection against reactor vessel failure 
    due to brittle fracture concerns under all postulated circumstances, 
    and (2) the revision to License Condition 2.C(3)(d) is 
    administrative to reflect the validity of the present analyses to 21 
    EFPY and (3) the revision to the Technical Specification Bases to 
    reflect the extension to 21 EFPY is an administrative change and 
    does not affect any activities or equipment in plant operation.
        3. Not involve a significant reduction in a margin of safety 
    because: (1) revision of the pressure-temperature curves and the 
    extended applicability of the pressurizer level/RCS pressure limit 
    curves maintains the present margin of safety from reactor vessel 
    brittle fracture as required by 10 CFR 50, Appendix G, and (2) the 
    revision to License Condition 2.C(3)(d) and the Bases revision are 
    administrative and do not affect any analyses which provide the 
    basis for the Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: Leif J. Norrholm
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: February 14, 1995
        Description of amendment request: The proposed change revises 
    Technical Specification 4.4.D to reference the testing requirements of 
    10 CFR Part 50, Appendix J, and to state that the Nuclear Regulatory 
    Commission-approved exemptions to the applicable regulatory 
    requirements are permitted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Virginia Electric and Power Company has performed an evaluation 
    of ... the proposed administrative Technical Specification change, 
    in accordance with 10 CFR 50.91(a)(1) regarding no significant 
    hazards considerations using the standards in 10 CFR 50.92(c). A 
    discussion of these standards as they relate to this ... amendment 
    request follows.
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The proposed change ... revises Technical Specification 4.4.D to 
    reference the testing frequency requirements of 10 CFR 50 Appendix J 
    and to state that NRC approved exemptions to the applicable 
    regulatory [[Page 14030]] requirements are permitted. The current 
    Technical Specification requires retests in accordance with Section 
    III.D.1(a) of Appendix J. The proposed administrative change simply 
    includes the statement ``as modified by NRC approved exemptions.'' 
    No new requirements are added, nor are any existing requirements 
    deleted. Any specific changes to the requirements of Section 
    III.D.1(a) will require a submittal from Virginia Electric and Power 
    Company under 10 CFR 50.12 and subsequent review and approval by the 
    NRC prior to implementation. The proposed change is stated 
    generically to avoid the need for further Technical Specification 
    changes if different exemptions are approved in the future.
        The proposed change, in itself, does not affect reactor 
    operations or accident analyses and has no radiological 
    consequences. The change provides clarification so that future 
    Technical Specifications changes will not be necessary to correspond 
    to applicable NRC approved exemptions from the requirements of 
    Appendix J.
        Therefore, this proposed change does not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The proposed Technical Specification amendment provides 
    clarification to a specification that paraphrases a codified 
    requirement.
        Since the proposed change would not change the design, 
    configuration or method of operation of the plant, it would not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The proposed Technical Specification change is administrative 
    and clarifies the relationship between the requirements of TS 4.4.D, 
    Appendix J, and any approved exemptions to Appendix J. It does not, 
    in itself, change a safety limit or [a] Limiting Condition for 
    Operation. The NRC will directly approve any proposed change or 
    exemption to III.D.1(a) of Appendix J prior to implementation.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, 951 E. Byrd Street, Richmond, Virginia 
    23219.
        NRC Project Director: David B. Matthews
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of amendment request: February 14, 1995
        Brief description of amendment request: The amendment request 
    proposes changes to Technical Specification 3.8.2, ``AC Sources-
    Shutdown;'' 3.8.5, ``DC Sources-Shutdown;'' and 3.8.8, ``Inverters-
    Shutdown.'' The proposed changes would revise the operability 
    requirements for the Division 3 diesel generator and the Division 3 and 
    4 batteries, battery chargers, and inverters to apply only when the 
    high pressure core spray system is required to be operable.Date of 
    publication of individual notice in Federal Register: February 17, 1995 
    (60 FR 9412).
        Expiration date of individual notice: March 20, 1995
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: September 8, 1994
        Brief description of amendment request: The amendment request 
    proposes changes to Technical Specification Section 3/4.9.1 to 
    establish administrative controls to address a possible boron dilution 
    event directly from the reactor makeup water system.
        Date of publication of individual notice in Federal Register: March 
    1, 1995 (60 FR 11151).
        Expiration date of individual notice: March 31, 1995
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket No. STN 50-529, Palo 
    Verde Nuclear Generating Station, Unit 2, Maricopa County, Arizona
    
        Date of application for amendment: November 30, 1994, as 
    supplemented by letter dated January 27, 1995
        Brief description of amendment: The amendment changed the 
    pressurizer code safety valve lift setting from 2500 
    [[Page 14031]] psia to 2475 psia. The lift setting is being changed to 
    permit Unit 2 to operate with up to 1500 plugged tubes in each steam 
    generator.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995
        Amendment No.: 78
        Facility Operating License No. NPF-74: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    496) The additional information contained in the January 27, 1995, 
    supplemental letter was clarifying in nature and thus within the scope 
    of the initial notice and did not affect the NRC staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated March 1, 1995.No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station,Plymouth County, Massachusetts
    
        Date of application for amendment: September 6, 1994
        Brief description of amendment: The proposed amendment relocates 
    the alarms for the drywell to suppression chamber vacuum breaker to a 
    different annunicator panel.
        Date of issuance: February 16, 1995 Effective date: To be 
    implemented prior to startup from refueling outage 10.
        Amendment No.: 158
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 26, 1994 (59 FR 
    53839) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of application for amendments: January 5, 1994, as 
    supplemented by letters dated April 26, 1994, September 30, 1994, and 
    January 12, 1995.
        Brief description of amendments: The amendments change the 
    Braidwood Technical Specifications to remove the requirement to verify, 
    every 18 months, that the control room ventilation can be manually 
    isolated.
        Date of issuance: February 28, 1995
        Effective date: February 28, 1995
        Amendment Nos.: 60 and 60
        Facility Operating License Nos. NPF-72 and NPF-77: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 25, 1995 (60 FR 
    4930). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 28, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Wilmington Township Public 
    Library, 201 S. Kankakee Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IllinoisDocket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: August 31, 1993, as 
    supplemented July 19, 1994.
        Brief description of amendments: The amendments revise the 
    technical specifications by increasing the allowed outage time for an 
    inoperable chiller only in MODES 1 through 4, adding an optional ACTION 
    statement in MODES 5 and 6, and adding a surveillance requirement for 
    the control room ventilation system.
        Date of issuance: March 2, 1995
        Effective date: March 2, 1995
        Amendment Nos.: 70, 70, 61 and 61
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 25, 1995 (60 FR 
    4932). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 2, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.Commonwealth Edison Company, Docket 
    Nos. 50-237 and 50-249, Dresden Nuclear Power Station, Units 2 and 3, 
    Grundy County, Illinois; Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, IllinoisDate 
    of application for amendments: July 29, 1992, as supplemented January 
    14, 1993, and February 16, 1993
        Brief description of amendments: Dresden and Quad Cities Technical 
    Specification Upgrade Program. Date of issuance: February 16, 
    1995Effective date: Immediately, to be implemented by December 31, 
    1995.
        Amendment Nos.:  131, 125, 152, and 148
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34071) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 16, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: For Dresden, The Morris Public 
    Library, 604 Liberty Street, Morris, Illinois 60450; For Quad Cities, 
    The Dixon Public Library, 221 Hennepin Avenue, Dixon, Illinois 61021.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of application for amendments: July 29, 1992, as supplemented 
    January 14, 1993, February 16, 1993 and January 27, 1995
        Brief description of amendments: The July 29, 1992, application, is 
    one of twelve applications which have been submitted by Commonwealth 
    Edison Company (ComEd) in an effort to upgrade the existing custom 
    Technical Specifications (TS) to the Boiling Water Reactor (BWR) 
    Standard Technical Specifications (STS). Dresden has recently 
    rescheduled the Unit 2 refueling outage from March 4, 1995, until June 
    1995. Currently, the surveillance frequency for certain Inservice 
    Testing (IST) requirements expires on February 21, 1995. The current 
    TSs do not make provisions for a grace period for surveillance 
    frequencies of the IST program. In accordance with BWR STS guidance, 
    the TSs regarding IST proposed in the July 29, 1992, application, allow 
    the flexibility to perform these tests appropriately during refueling 
    outages (where applicable) by providing a 25 percent extension to IST 
    surveillance intervals. The January 27, 1995, supplement requested the 
    staff to review and approve just that portion of the July 29, 1992, 
    application dealing with the implementation of the IST program in 
    Section 3.0/4.0 of the proposed TS. [[Page 14032]] 
        Date of issuance: February 22, 1995Effective date: February 22, 
    1995
        Amendment Nos.:  132 and 126
        Facility Operating License Nos. DPR-19 and DPR-25: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34071) The January 27, 1995, letter did not change the initial proposed 
    no significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation datedFebruary 22, 1995.No significant hazards consideration 
    comments received: No
        Local Public Document Room location: Morris Public Library, 604 
    Liberty Street, Morris, Illinois 60450.
    
    Connecticut Yankee Atomic Power Company and Northeast Nuclear 
    Energy Company, Docket Nos. 50-213 and 50-245, Haddam Neck Plant 
    and Millstone Nuclear Power Station, Unit 1, Middlesex County and 
    New London County, Connecticut
    
        Date of application for amendments: October 31, 1994, as 
    supplemented February 14, 1995.
        Brief description of amendments: The amendments renew the existing 
    license conditions for both plants to implement and maintain Integrated 
    Implementation Schedule Program Plans (the Program Plans). The Program 
    Plans provide a methodology to be followed for scheduling plant 
    modifications and engineering evaluations.
        Date of issuance: February 23, 1995
        Effective date:  February 23, 1995
        Amendment Nos.:  183 for Haddam Neck, 80 for Millstone 1
        Facility Operating License Nos. DPR-61 and DPR-21. Amendments 
    revise the Licenses.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63117)The February 14, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated February 23, 
    1995.No significant hazards consideration comments received: No.
        Local Public Document Room locations: Russell Library, 123 Broad 
    Street, Middletown, CT 06457, for the Haddam Neck Plant, and the 
    Learning Resource Center, Three Rivers Community-Technical College, 
    Thames Valley Campus, 574 New London Turnpike, Norwich, CT 06360, for 
    Millstone Unit 1.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of application for amendment: October 5, 1994, as supplemented 
    February 10, 20, and 22, 1995.
        Brief description of amendment: The amendment revises primary 
    coolant system (PCS) pressure-temperature limits, power-operated relief 
    valve setting limits, and primary coolant pump starting limits to 
    accommodate reactor vessel fluence for an additional 4 effective full 
    power years. The amendment also revises the emergency core cooling 
    system technical specifications to render two high-pressure safety 
    injection pumps incapable of injecting into the PCS when the PCS is 
    below 300 deg.F rather than rendering both inoperable below 260 deg.F. 
    In addition, it revises the pressurizer heatup to achieve consistency 
    between design assumptions and technical specifications limits.
        Date of issuance: March 2, 1995
        Effective date: March 2, 1995
        Amendment No.: 163
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    501) The February 10, 20, and 22, 1995, submittals provided 
    clarifyinginformation which was within the scope of the initial 
    application and did not affect the staff's initial proposed no 
    significant hazards consideration findings. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    March 2, 1995.No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: January 10, 1994, as 
    supplemented March 21 and September 15, 1994, and January 5, 1995
        Brief description of amendments: The amendments revised Technical 
    Specification Table 2.2-1 and TS 4.2.5 to allow a change in the method 
    for measuring reactor coolant system (RCS) flow rate from the 
    calorimetric heat balance method to a method based on a one-time 
    calibration of the RCS cold leg elbow differential pressure taps.
        Date of issuance: February 17, 1995
        Effective date: To be implemented within 30 days from the date of 
    issuance
        Amendment Nos.: 128 and 122
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 26, 1994 (59 FR 
    3743) for Unit 1; and March 1, 1994 (59 FR 9785) for Unit 2
        The March 21 and September 15, 1994, and January 5, 1995, letters 
    provided additional information that did not change the initial scope 
    of the January 10, 1994, application and the initial proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 17, 1995. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear 
    One,Unit No. 1, Pope County, Arkansas
    
        Date of amendment request: August 30, 1994
        Brief description of amendment: The amendment revised the Technical 
    Specifications to address the installation of two battery chargers on 
    each 125 vdc power train in lieu of the ``swing'' battery charger that 
    is currently used.
        Date of issuance: February 17, 1995
        Effective date: February 17, 1995
        Amendment No.: 176
        Facility Operating License No. DPR-51. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 17, 1995 (60 FR 
    3439) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 17, 1995.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear 
    One,Unit No. 1, Pope County, Arkansas
    
        Date of amendment request: June 22, 1994.
        Brief description of amendment: The amendment extends the allowable 
    outage time for one inoperable train of emergency feedwater from 36 
    hours to 72 hours, clarifies the specifications and their associated 
    bases, and relocates information within the specifications.
        Date of issuance: March 1, 1995
        Effective date: 30 days following the date of 
    issuance. [[Page 14033]] 
        Amendment No.: 177
        Facility Operating License No. DPR-51. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994, (59 FR 
    42339) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 1, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: January 19, 1995
        Brief description of amendment: The amendment changed the Appendix 
    A technical specifications (TSs) by adding TS 3.0.5 and its associated 
    Bases. This new specification will allow equipment removed from service 
    or declared inoperable to comply with ACTIONS to be returned to service 
    under administrative controls soley to perform testing required to 
    demonstrate its OPERABILITY or the OPERABILITY of other equipment.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995
        Amendment No.: 101
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 27, 1995 (60 FR 
    5441) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 1, 1995.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: August 11, 1994, as supplemented by 
    letter dated December 2, 1994.
        Brief description of amendment: The amendment revised the Technical 
    Specifications for the Waterford Steam Electric Station, Unit 3, by 
    modifying the specifications having cycle-specific parameter limits by 
    replacing the values of those limits with a reference to a core 
    operating limits report for the values of those limits. These changes 
    are in accordance with the requirements of Generic Letter 88-16.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995
        Amendment No.: 102
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65812) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 1, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: August 19, 1994, as supplemented by 
    letter dated October 14, 1994.
        Brief description of amendment: The amendment changed the Appendix 
    A technical specification (TSs) by removing the Limiting Condition For 
    Operation (LCO) 3/4.3.4, the associated surveillance requirements, and 
    Bases information from the TSs. This information and requirements will 
    be incorporated into the Waterford 3 Updated Final Safety Analysis 
    Report (UFSAR) and maintained under the provisions of 10 CFR 50.59.
        Date of issuance: March 2, 1995
        Effective date: March 2, 1995
        Amendment No.: 103
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45023) The additional information contained in the supplemental letter 
    dated October 14, 1994, was clarifying in nature and thus, within the 
    scope of the initial notice and did not affect the staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated March 2, 1995.No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company,Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: April 21, 1993
        Brief description of amendment: The amendment revised the 
    requirement for control rod testing to increase the ``notch testing'' 
    surveillance interval for partially withdrawn control rods from once 
    per 7 days to once per 31 days. The change is consistent with the 
    format and content of the Improved Standard Technical Specifications 
    (NUREG-1434, Revision 0).
        Date of issuance: February 16, 1995
        Effective date: February 16, 1995
        Amendment No: 115
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 12, 1993 (58 FR 
    28055) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 16, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, Mississippi 39120.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company,Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: July 14, 1993
        Brief description of amendment: The amendment revised technical 
    specification requirements for the hydrogen ignition system (HIS). The 
    amendment also removed several tables related to the HIS in accordance 
    with guidance contained in Generic Letter 91-08, ``Removal of Component 
    Lists From Technical Specifications.''
        Date of issuance: February 16, 1995
        Effective date: February 16, 1995
        Amendment No: 116
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46232) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 16, 1995. No 
    significant hazards consideration comments received: No [[Page 14034]] 
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce at Washington, Natchez, Mississippi 39120.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company,Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: August 11, 1993
        Brief description of amendment: The amendment deleted the 
    requirements of Limiting Condition for Operation (LCO) 3.3.3.9 and 
    Surveillance Requirement 4.3.3.9 related to loose-part detection 
    instrumentation. The deleted requirements will be relocated to 
    documents that are controlled by the licensee under the provisions of 
    10 CFR 50.59. The change is consistent with the format and content of 
    the Improved Standard Technical Specifications (NUREG-1434, Revision 
    0).
        Date of issuance: February 16, 1995
        Effective date: February 16, 1995
        Amendment No: 117
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46232) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 16, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, Mississippi 39120.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company,Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: August 11, 1993
        Brief description of amendment: The amendment deleted certain 
    accident monitoring instruments from Technical Specification Table 
    3.3.7.5-1 ``Accident Monitoring Instrumentation'' and deleted the 
    corresponding Surveillance Requirements from Table 4.3.7.5-1, 
    ``Accident Monitoring Instrumentation Surveillance Requirements.'' The 
    deleted requirements will be relocated to documents that are controlled 
    by the licensee under the provisions of 10 CFR 50.59. The change is 
    consistent with the format and content of the Improved Standard 
    Technical Specifications (NUREG-1434, Revision 0).
        Date of issuance: February 16, 1995
        Effective date: February 16, 1995
        Amendment No: 118
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46234) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 16, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, Mississippi 39120.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company, Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: October 22, 1993, as 
    supplemented by letters dated February 10, and 14, 1995.
        Brief description of amendment: The amendment modified the testing 
    frequencies for the drywell bypass test and the airlock test, relocated 
    certain drywell airlock tests from the technical specifications to 
    administrative procedures, and incorporates various improvements from 
    the Improved Standard Technical Specifications (NUREG-1434, Revision 
    0).
        Date of issuance: February 16, 1995
        Effective date: February 16, 1995
        Amendment No: 119
        Facility Operating License No. NPF-29. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64607) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 16, 1995. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, Mississippi 39120.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: May 17, 1993, as supplemented on 
    December 23, 1994
        Brief description of amendment: The amendment changes the action 
    statement for inoperable degraded grid and loss of voltage relays and 
    their associated auxiliary relays and timers.
        Date of issuance: January 31, 1995
        Effective date: January 31, 1995
        Amendment No.: 193
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59750). The December 23, 1994, letter provided additional 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of this amendment is contained in a Safety Evaluation dated 
    January 31, 1995. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, PA 17105. The above Notice was to be 
    published in the Federal Register of February 15, 1995. The notice that 
    was inadvertently published at 60 FR 8762 relates to a licensing action 
    which has not been completed.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: November 7, 1994, as supplemented by 
    letters dated December 20, 1994, and January 23, 1995.
        Brief description of amendments: The amendments changed the number 
    of standby diesel generators (SDGs) (emergency power source) required 
    to be operable during Mode 6 with greater than or equal to 23 feet of 
    water above the reactor vessel flange, from two to one. The amendment 
    also allows limited substitution of an alternate onsite emergency power 
    source for one of the two required SDGs, in Mode 5, and in Mode 6 with 
    less than 23 feet of water. In addition, certain system specifications 
    that are affected by the changes for the emergency power source were 
    also changed.
        Date of issuance: February 14, 1995
        Effective date: February 14, 1995, to be implemented within 31 days 
    of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 34; Unit 2 - Amendment No. 
    20
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical [[Page 14035]] Specifications.Public comments 
    requested as to proposed no significant hazards consideration: Yes (60 
    FR 5739, dated January 30, 1995). The notice provided an opportunity to 
    submit comments on the Commission's proposed no significant hazards 
    consideration determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by March 1, 1995, 
    but stated that, if the Commission makes a final no significant hazards 
    consideration determination, any such hearing would take place after 
    issuance of the amendments.
        The Commission's related evaluation of the amendments, finding of 
    exigent circumstances, and final determination of no significant 
    hazards consideration is contained in a Safety Evaluation dated 
    February 14, 1995.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of application for amendment: August 15, 1994, as supplemented 
    on December 21, 1994, and January 20, 1995. The licensee's submittals 
    of December 21, 1994, and January 20, 1995, provided clarification and 
    did not change the original no significant hazards consideration.
        Brief description of amendment: The proposed amendment would revise 
    the Technical Specifications by increasing the allowable main steam 
    isolation valve (MSIV) leakage and deleting the requirements applicable 
    to the MSIV leakage control system.
        Date of issuance: February 22, 1995
        Effective date: February 22, 1995 and to be implemented within 90 
    days.
        Amendment No.: 207
        Facility Operating License No. DPR-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47169) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 22, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: August 12, 1994, as supplemented 
    on October 14, 1994 and February 6, 1995.
        Brief description of amendment: The amendment modifies Clinton 
    Power Station Technical Specification 3.6.5.1, ``Drywell,'' to permit a 
    one-time only change to forego performance of the drywell bypass 
    leakage rate test during the fifth refueling outage scheduled to begin 
    in March 1995.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995
        Amendment No.: 96
        Facility Operating License No. NPF-62. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49427). The October 14, 1994, and February 6, 1995, submittals 
    consisted of revisions and clarifications which did not change the 
    staff's initial proposed no significant hazards consideration 
    determination or expand the scope of the original notice.The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated March 1, 1995. No significant hazards 
    consideration comments received: No
        Local Public Document Room location:  The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments:  November 18, 1994
        Brief description of amendments: The amendments revise Technical 
    Specification 4.0.5 to delete the wording ``except where specific 
    written relief has been granted by the Commission pursuant to 10 CFR 
    50, Section 50.55a(g)(6)(i).'' This change allows the licensee to 
    implement certain 10 CFR 50.55a relief requests while the relief 
    requests are being reviewed by the NRC at the beginning of an updated 
    interval.
        Date of issuance: February 23, 1995
        Effective date: February 23, 1995
        Amendment Nos.: 190/176
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65817) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 23, 1995. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    MillstoneNuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: May 18, 1994
        Brief description of amendment: The amendment modifies the 
    operability requirements for the fuel building exhaust filter system. 
    The amendment will result in modifications to the applicability, 
    surveillance requirement, and bases sections of Technical Specification 
    3/4.9.12, ``Fuel Building Exhaust Filter System.''
        Date of issuance: February 22, 1995
        Effective date: As of the date of issuance to be implemented 
    within30 days.
        Amendment No.: 105
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 22, 1994 (59 FR 
    32234) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 22, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    DiabloCanyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County,California
    
        Date of application for amendments: July 9, 1992
        Brief description of amendments: The amendments extend the 
    operating licenses for the Diablo Canyon Nuclear Power Plant, Units 1 
    and 2 to recover or recapture the construction period of the reactors. 
    Specifically, the amendments extend the expiration date of the Unit 1 
    license from April 23, 2008, to September 22, 2021, and the expiration 
    date of the Unit 2 license from December 9, 2010, to April 26, 2025.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995
        Amendment Nos.: 97 and 96
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the license.
        Date of initial notice in Federal Register: July 22, 1992 (57 FR 
    32575) [[Page 14036]] The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated March 1, 1995.No 
    significant hazards consideration comments received: Yes. Comments from 
    the San Luis Obispo Mothers for Peace (MFP) and their contentions were 
    admitted into this proceeding. These contentions concern the adequacy 
    of the licensee's maintenance and surveillance program and interim 
    corrective actions in lieu of Thermo-Lag. The Atomic Safety and 
    Licensing Board, in its initial decision dated November 4, 1994 (LBP-
    94-35), authorized the staff to extend the DCPP operating license 
    expiration dates. Because a hearing was held prior to license issuance, 
    the staff does not need to make a final no significant hazards 
    consideration determination.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Pennsylvania Power and Light Company, Docket No. 50-387, 
    Susquehanna Steam Electric Station, Unit 1, Luzerne County, 
    Pennsylvania
    
        Date of application for amendment: July 27, 1994, as supplemented 
    October 27, 1994 and February 3, 1995
        Brief description of amendment: The amendment raises the authorized 
    Power Level from 3293 MWt to a new limit of 3441 MWt.
        Date of issuance: February 22, 1995
        Effective date: As of date of issuance and is to be implemented 
    prior to startup in Cycle 9, currently scheduled to occur in May 1995.
        Amendment No.: 143
        Facility Operating License No. NPF-14: This amendment revised the 
    Technical Specifications and license.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47171) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 22, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: June 23, 1994
        Brief description of amendments: The amendment revises Technical 
    Specification 4.0.5, which provides the requirements for inservice 
    inspection and testing of ASME Code components, to conform to Standard 
    Technical Specifications (NUREG-1433).
        Date of issuance: February 28, 1995
        Effective date: February 28, 1995
        Amendment Nos.: 144 and 113
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39595) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 28, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: October 28, 1994, and 
    supplemented by letter dated December 29, 1994
        Brief description of amendments: These amendments change the 
    Technical Specifications (TS) for the two units by adding reference 
    20 (Unit 1) and reference 18 (Unit 2) to Section 
    6.9.3.2 as ``PL-NF-90-001, Supplement 1, 'Application of Reactor 
    Analysis Methods for BWR Design and Analysis: Loss of Feedwater Heating 
    Changes and Use of RETRAN MOD 5.1,' September 1994.'' These additions 
    reflect changes to the methodology that the licensee is using to 
    perform its nuclear fuel reload analysis for the two units.
        Date of issuance: February 28, 1995
        Effective date: February 28, 1995
        Amendment Nos.: 145 and 114
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65819) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 28, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: August 31, 1994
        Brief description of amendments: These amendments address Section 
    5, ``Remove Temperature Requirement for Operational Condition 5 (TSCR 
    94-44-0), by revising TS Table 1.2 and TS Bases 3/4.9.11 to remove the 
    average reactor coolant temperature requirement in Operational 
    Condition (OPCON) 5, Refueling.
        Date of issuance: January 27, 1995
        Effective date: January 27, 1995Amendment Nos. 88 and 50
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55884) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 27, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment:  November 16, 1994
        Brief description of amendment: The amendment revises Technical 
    Specifications Section 3.10.8 and the associated Bases, to reduce the 
    maximum allowable control rod drop time from 2.4 to 1.8 seconds.
        Date of issuance: February 21, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 160
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 20, 1995 (60 FR 
    4203) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 21, 1995.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610. [[Page 14037]] 
    
    Saxton Nuclear Experimental Corporation, Docket No. 50-146, Saxton 
    Nuclear Reactor Facility
    
        Date of application for amendment: August 8, 1994, as supplemented 
    on October 28, 1994, and January 12, 1995.
        Brief description of amendment: The amendment adds characterization 
    as an authorized activity at Saxton and improves the wording of the 
    technical specifications.
        Date of issuance: February 22, 1995
        Effective date: February 22, 1995
        Amendment No.: 12Amended Facility License No. DPR-4: Amendment 
    changed the Technical Specifications
        Date of initial notice in Federal Register: November 9, 1994. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated February 22, 1995.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: December 30, 1993, as 
    supplemented by letters dated June 3, 1994, August 25, 1994, and 
    January 3, 19, and 30, 1995.
        Brief description of amendments: These amendments revise TS 3.9.4, 
    ``Containment Building Penetrations,'' and the associated bases to 
    allow both doors of the containment personnel airlock to be open at the 
    same time during refueling operations provided certain conditions are 
    met.
        Date of issuance: February 28, 1995
        Effective date: February 28, 1995
        Amendment Nos.: 117 and 106
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49434). The additional information contained in the January 3, 19, 
    and 30, 1995, letters were clarifying in nature, within the scope of 
    the initial notice and did not affect the NRC staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated February 28, 1995.No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama.
    
        Date of amendments request: December 19, 1994
        Brief description of amendments: The amendments to Technical 
    Specifications include: (1) a revision in Table 3.7-3 to the main steam 
    safety valve (MSSV) setpoint tolerance from plus or minus 1 percent to 
    plus or minus 3 percent, (2) modification of the bases to 3/4.7.1.1 to 
    increase the relieving capacity of the MSSVs to at least 12,984,660 
    pounds per hour which corresponds to approximately 112 percent of total 
    secondary steam flow at 100 percent rated thermal power, (3) 
    modifications to Table 3.7-1 to reduce the allowable power range 
    neutron flux high setpoints for multiple inoperable steam generator 
    safety valves, and (4) an editorial correction to Bases 3/4.7.1.2 to 
    indicate required auxiliary feedwater flow at ``1133 psia'' rather than 
    ``1133 psig.''
        Date of issuance March 1, 1995
        Effective date: March 1, 1995
        Amendment Nos.: 112 and 103
        Facility Operating License Nos. NPF-2 and NPF-8. Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    505) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 1, 1995No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated March 1, 1995No significant hazards 
    consideration comments received: No
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: September 29, 1993
        Brief description of amendment: The proposed changes increase the 
    amount of boron required in the standby liquid control system.
        Date of issuance: February 28, 1995
        Effective date: February 28, 1995
        Amendment Nos.: 217, 233 and 191
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29635) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 28, 1995.No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Athens Public library, South 
    Street, Athens, Alabama 35611
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: September 30, 1993 (TS 336)
        Brief description of amendment: The proposed changes revise and 
    clarify the spent fuel pool water level, temperature, sampling, and 
    analysis surveillance requirements.
        Date of issuance: March 2, 1995
        Effective date: March 2, 1995
        Amendment Nos.: 218, 334 and 192
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67862) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 2, 1995.No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Athens Public library, South 
    Street, Athens, Alabama 35611
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: March 31, 1994
        Brief description of amendment: For Browns Ferry Units 1 and 3, the 
    proposed changes provide for operation in the extended load line limit 
    region and revised rod block monitor operability requirements. For all 
    three Browns Ferry units, the changes delete a obsolete value for rated 
    loop recirculation flow rate, relocate cycle-specific equations to the 
    Core Operating Limits report, and provide other miscellaneous changes.
        Date of issuance: February 24, 1995
        Effective date: February 24, 1995
        Amendment Nos.: 216, 232, 190
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49437) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 24, 1995.No significant 
    hazards consideration comments received: None [[Page 14038]] 
        Local Public Document Room location: Athens Public library, South 
    Street, Athens, Alabama 35611
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: October 7, 1994
        Brief description of amendment: Eliminates redundancy in system 
    leakage test requirements by revising TS 3/4.5.2 and its associated 
    basis for the Emergency Core Cooling System and TS 3/4.6.2 and its 
    associated basis for the Containment Spray System.
        Date of issuance: February 27, 1995
        Effective date: February 27, 1995 and to be implemented within 90 
    days.
        Amendment No. 195
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55893) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 27, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: November 18, 1994 (published in Federal 
    Register as November 11, 1994)
        Brief description of amendments: The proposed amendments would 
    provide for cycle-specific allowances to account for increases in the 
    Heat Flux Hot Channel Factor between monthly surveillances.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995, to be implemented within 30 days of 
    issuance.
        Amendment Nos.: Unit 1 - Amendment No. 34; Unit 2 - Amendment No. 
    20
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63127) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 1, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: October 31, 1994
    
        Brief description of amendment: The amendment modifies the Techical 
    Specifications (TS) to (1) add two action statements that would provide 
    allowed outage times for either one or both of the scram discharge 
    volume (SDV) vent or drain valves less stringent than the current 
    requirements of TS 3.0.3., and (2) change the surveillance requirements 
    for the SDV vent and drain valves to conduct the testing during 
    shutdown conditions rather than at power as currently required.
        Date of issuance: February 27, 1995
        Effective date: February 27, 1995
        Amendment No.: 134
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65828) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 27, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    NuclearPower Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: February 23, 1994
        Brief description of amendment: The amendment revises Kewaunee 
    Nuclear Power Plant (KNPP) Technical Specification (TS) 6.8.c by 
    removing the requirement to conduct a biennial review of plant 
    procedures in accordance with American National Standards Institute 
    (ANSI) N18.7-1976, Section 5.2.15. Alternate programs that are 
    described in the KNPP Operational Quality Assurance Program Description 
    (OQAPD) will be used to ensure that procedures are reviewed and 
    maintained current.
        Date of issuance: February 23, 1995
        Effective date: February 23, 1995 and to be implemented within 30 
    days.
        Amendment No.: 115
        Facility Operating License No. DPR-43. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14903) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 23, 1995.No significant 
    hazards consideration comments received: None.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for [[Page 14039]] example, in derating or shutdown of a 
    nuclear power plant or in prevention of either resumption of operation 
    or of increase in power output up to the plant's licensed power level, 
    the Commission may not have had an opportunity to provide for public 
    comment on its no significant hazards consideration determination. In 
    such case, the license amendment has been issued without opportunity 
    for comment. If there has been some time for public comment but less 
    than 30 days, the Commission may provide an opportunity for public 
    comment. If comments have been requested, it is so stated. In either 
    event, the State has been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By April 14, 1995, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear [[Page 14040]] Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Pennsylvania Power and Light Company, Docket No. 50-388, 
    SusquehannaSteam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendment: February 7, 1995
        Brief description of amendment: The amendment changed the Technical 
    Specifications to allow continued operation with one neutron flux 
    monitor system channel (B'' channel) inoperable and should 
    the remaining channel become inoperable to allow continued plant 
    operation for 7 days to restore one of the two inoperable channels.
        Date of issuance: March 1, 1995
        Effective date: March 1, 1995
        Amendment No.: 115
        Facility Operating License No. NPF-22: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. On February 8, 1995, the staff 
    issued a Notice of Enforcement Discretion, which was immediately 
    effective and remained in effect until this amendment was issued.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances, consultation with the Commonwealth of 
    Pennsylvania and final no significant hazards considerations 
    determination are contained in a Safety Evaluation dated March 1, 1995.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge 2300 N Street NW., Washington, D.C. 20037
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18071.
        NRC Project Director: John F. Stolz
        Dated at Rockville, Maryland, this 8th day of March 1995.
        For the Nuclear Regulatory Commission
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects - III/IV, Office of 
    Nuclear Reactor Regulation
    [Doc. 95-6207 Filed 3-14-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Effective Date:
3/1/1995
Published:
03/15/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X95-60315
Dates:
March 1, 1995
Pages:
14015-14040 (26 pages)
PDF File:
x95-60315.pdf