94-6412. Pennsylvania Power and Light Co., et al.; Environmental Assessment and Finding of No Significant Impact  

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    [FR Doc No: 94-6412]
    
    
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    [Federal Register: March 18, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket No. 50-388]
    
     
    
    Pennsylvania Power and Light Co., et al.; Environmental 
    Assessment and Finding of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of an amendment to Facility Operating License No. 
    NPF-22, issued to Pennsylvania Power and Light Company, (the licensee), 
    for operation of the Susquehanna Steam Electric Station, Unit 2, 
    located in Luzerne County, Pennsylvania.
    
    Environmental Assessment
    
    Identification of Proposed Action
    
        This Environmental Assessment has been prepared to address 
    potential environmental issues related to the licensee's application of 
    November 24, 1993, as supplemented January 7, 1994, to amend the 
    Susquehanna, Unit 2 operating license. The proposed amendment would 
    increase the licensed core thermal power from 3293 MWt to 3441 MWt, 
    which represents an approximate increase of 4.5% over the current 
    licensed power level.
        The proposed action involves NRC issuance of a license amendment to 
    uprate the authorized power level by changing the operating license, 
    including Appendix A of the license (Technical Specifications). No 
    change is needed to Appendix B of the license (Environmental Protection 
    Plan--Nonradiological).
    
    The Need for the Proposed Action
    
        The proposed action is needed to permit an increase in the licensed 
    core thermal power from 3293 MWt to 3441 MWt and provide the licensee 
    with the flexibility to increase the potential electrical output of 
    Susquehanna, Unit 2, providing additional electrical power to service 
    domestic and commercial areas of the Pennsylvania Power and Light 
    (PP&L) Company and Allegheny Electric Cooperative, Inc. grid.
    
    Environmental Impacts of the Proposed Action
    
        The ``Final Environmental Statement (FES) related to operation of 
    Susquehanna Steam Electric Station, Units 1 and 2'' was issued June 
    1981 (NUREG-0564). By letter of June 15, 1992, the licensee submitted 
    ``Licensing Topical Report NE-092-001 for Power Uprate With Increased 
    Core Flow'' for Susquehanna Steam Electric Station (SSES), Units 1 and 
    2. The report was submitted to support future proposed amendments to 
    Units 1 and 2 licenses to permit up to a 4.5-percent increase in 
    reactor thermal power and an 8-percent increase in core flow for each 
    unit. The NRC approved the topical report by letter of November 30, 
    1993. The licensee submitted the proposed amendment to implement power 
    uprate for Unit 2 by the letter of November 24, 1993, which is the 
    subject of this environmental assessment. The licensee expects to 
    submit a similar application for Unit 1 within the next year. Section 
    11.4 of the above Topical Report provided an environmental assessment 
    of the proposed power uprate, including projected nonradiological 
    environmental effects and radiological effects from postulated 
    accidents. Sections 8.1, 8.2 and 8.3 of the Topical Report discussed 
    the potential effect of power uprate on the liquid, gaseous and solid 
    radwaste systems. Sections 8.4, 8.5 and 8.6 discussed the potential 
    effect of power uprate on radiation sources within the plant and 
    radiation levels from normal and post-accident operation. Section 9.2 
    of the Topical Report presented the results of the calculated whole 
    body and thyroid doses at uprated power vs. current authorized power 
    conditions at the exclusion area boundary and the low population zone 
    (LPZ) that might result from the postulated design basis radiological 
    accidents [i.e., loss-of-coolant accident (LOCA), main steam line break 
    accident (MSLBA) outside containment, fuel handling accident (FHA) and 
    control rod drop accident (CRDA)]. Other accidents (non-LOCA) that were 
    previously analyzed in the licensee's Final Safety Analysis Report 
    (FSAR) were also reassessed. All off-site radiological doses remain 
    well below established regulatory limits for power uprate operation.
        Supplemental information related to the non-radiological 
    environmental assessment was also presented in the licensee's letter of 
    February 7, 1994.
        The licensee summarized their reassessment of potential 
    radiological and non-radiological impacts of station operation at a 
    slightly higher power level as follows:
    
    Non-Radiological Environmental Assessment
    
        Since power uprate will not significantly change the methods of 
    generating electricity, nor of handling any influents from the 
    environment or effluents to it, no new or different environmental 
    impacts are expected. The conservative models and methods used in 
    the environmental assessments of the original design, confirmed by 
    studies conducted during actual operation, show that more than 
    adequate margin exists for the proposed power uprate without 
    exceeding the nonradiological environmental effects estimated in the 
    original estimates and analyses and cited in the original permit 
    applications and impact statements.
        The maximum withdrawal rate from the river will increase from 
    the current value of 38,800 gpm to 40,700 gpm after power uprate, an 
    increase of 5%. The maximum blowdown rate will increase from the 
    current value of 10,300 gpm to 10,800 gpm, an increase of 5%.
        After reviewing the additional water withdrawal requirements and 
    increased blowdown rate from the natural draft cooling towers at the 
    Susquehanna SES (SSES) associated with power uprate, PP&L determined 
    that there will be no adverse effects to the river flow or river 
    biota. This conclusion is based on two factors. First, the projected 
    number of fish estimated to be impinged per day would increase from 
    20 to 21 and the number of larvae estimated to be entrained would 
    increase by only 13,000 to 363,000 per day. Biologically, these 
    estimated increases represent a negligible impact to the river 
    ecosystem. Second, the maximum cooling tower blowdown flow after 
    power uprate is estimated to increase by only 5% which amounts to 
    500 gpm. This amounts to less than .5% of the average river flow.
        The cooling blowdown from the cooling tower basin is through a 
    diffuser into the river. The characteristics of the cooling tower 
    are such that there is greater air flow through the tower caused by 
    the higher circulating water return temperature at power uprate 
    conditions. This increased air flow removes the additional heat load 
    resulting in negligible cooling tower basin temperature changes.
        Estimates, assuming that both SSES cooling towers are operating 
    at the original 100% power level for a year, would result in 58,000 
    pounds of solids per year as salt drift, spread over a large area. 
    Modelling indicated the heaviest localized deposition of solids 
    would be 3 pounds/acre/year (SSES Environmental Report section 
    5.3.4). The power uprate should have no impact on these estimates, 
    especially with the conversatism built into the model by assuming 
    100% capacity factor. Note also that the design cooling tower drift 
    is a function of circulating water flow which is not changing for 
    power uprate.
        Studies on the possible effects of salt drift have been 
    conducted at the SSES since 1977. These studies have included 
    monthly examination of natural vegetation during the growing season 
    (1977 to date), annual quantitative vegetation studies (1977 to 
    date), a two-year study on the effect of simulated salt drift on 
    corn and soybeans (1985-86), and annual forest inspections since 
    1982.
        The monthly examinations have utilized several transects (salt 
    drift transects) in the vicinity of the power station for possible 
    salt damage to natural vegetation and incidence of parasitic plant 
    diseases. The annual vegetation studies consider possible long-term 
    changes in forest utilized salt spray approximating the composition 
    of the cooling tower drift from the SSES at ``worst case'' 
    concentration on agricultural crops in two fields.
        None of the studies have found evidence for damage to 
    agricultural crops or natural vegetation from salt drift. It should 
    be noted that the water used at the SSES (from the Susquehanna 
    River) does not contain the same salts as brackish water used at 
    estuarine coo[l]ing tower[s]; its effects are more like plant 
    micronutrients. The natural vegetation studies over 15 years have 
    found no salt drift damage and plant diseases in accordance with 
    host presence and location. The simulated salt drift studies 
    utilized concentrations estimated at 5 and 10 times maximum salt 
    drift concentration in the SSES plume. It is therefore unlikely that 
    salt drift damage would occur from an approximate 5% consumptive 
    rise in water usage.
        There will be no changes to the cooling tower water chemistry as 
    a result of power uprate. The pre-uprate levels of cycles of 
    concentration will be maintained. Since there will be a 5% increase 
    in blowdown flow, there will be a 5% increase in chemical discharge 
    to the river.
        The velocity of the intake water will increase by 5% to .37 ft/
    sec with power uprate which is below the recommended intake design 
    velocity of 0.5 ft/sec.
        Sound level monitoring was conducted at both near site (less 
    than 1 mile) and far site locations (greater than 1 mile) from the 
    Susquehanna SES site from 1972 and 1985. This survey was conducted 
    prior to and during construction and during one and two unit 
    operation. The tow Cooling Towers were identified to be one of the 
    major site nose sources. The cumulative effects of all noise sources 
    associated with station operation were determined to be less than 
    the U.S. Environmental Protection Agency recommended day-night 
    equivalent sound level limit of 55 dBA at all monitoring locations. 
    It is not expected that this level will be exceeded at any of the 
    locations with the possible exception of an area approximately 2,200 
    feet southeast of the Cooling Towers where the measured sound level 
    including a nighttime weighting factor of +10 dBA was 54 DBA. Sound 
    levels will be monitored at power uprate conditions.
        As indicated previously, water discharge flow from power uprate 
    may increase 5% above the design discharge rate to 10,800 gpm. This 
    is well below the maximum flow of 16,000 gpm reviewed in the SSES 
    Environmental Report (Table 3.3-1) and, therefore, the additional 
    flow from power uprate is not considered to be an adverse impact to 
    the river.
        At the Susquehanna SES cooling tower blowdown discharges into 
    the river through a diffuser pipe located on the river bottom. 
    Velocity of this discharge was calculated in Appendix G, Thermal 
    Discharge, Response 1, pages THE-1.1 and 1.2 of the Environmental 
    Report. Water discharges through 72-4'' ports into the river. The 
    velocity associated with a 10,000 gpm discharge was calculated to be 
    5.83 fps and rounded to 6 fps. This rounded off value was used when 
    preparing [the] SSES Environmental Report. The velocity associated 
    with a 10,800 gpm discharge is also approximately 6 fps.
        Thermal plume studies conducted in the fall, winter, and spring 
    of 1986-87 indicated a maximum temperature rise of 1 deg.F within an 
    80 foot mixing zone from the diffuser pipe. Present Pennsylvania 
    Department of Environmental Resources water quality criteria states 
    that ambient river temperature rise from thermal discharges shall 
    not cause the temperature in the receiving water body to rise more 
    than 2 deg.F in one hour. The thermal discharges from the cooling 
    tower blowdown from power uprate will not exceed this water quality 
    criteria.
        Chemical composition of the blowdown after power uprate will not 
    exceed the NPDES permit limits.
    
    The staff reviewed the potential effect of power uprate on plant makeup 
    water usage. There will be no significant increase in makeup water 
    requirements for any plant systems as a result of power uprate. This 
    includes the reactor coolant system, the condensate, feedwater and 
    steam systems, the emergency service water system, the reactor and 
    turbine building closed cooling water systems or any of the normal 
    service water systems. The only effect of power uprate on the component 
    cooling water system and turbine plant cooling water system from power 
    uprate is an increased heat load. The service water system removes heat 
    from the heat exchangers in the turbine, reactor and radwaste buildings 
    and transfers this heat to the cooling towers where it is dissipated. 
    The increased heat load on intermediate systems is reflected in the 
    discussion of potential impacts from increased cooling tower blowdown 
    and thermal discharges remain acceptable. Inventory makeup is not 
    affected. Makeup requirements for the auxiliary boiler, the fire 
    protection system or other auxiliary systems are unaffected by power 
    uprate.
        The licensee has stated that there are no changes required to the 
    SSES Environmental Protection Plan as a result of operation at uprated 
    power. Specifically, the licensee stated:
    
        Chapter 3, Consistency Requirements, section 3.1, Plant Design 
    Operations, of this plan discusses how proposed changes need to be 
    addressed. Through the PP&L Unreviewed Environmental Question 
    Program, changes such as that of power uprate will be reviewed.
        An ``Unreviewed Environmental Question'' evaluation was 
    conducted in accordance with each unit's ``Environmental Protection 
    Plan'' to determine if power uprate could cause any significant 
    environmental impacts. This included a review of the National 
    Pollutant Discharge Elimination System (NPDES) Permit and other 
    environmental permits, and indicated that power uprate should not 
    contribute to any new noncompliances. No significant increase in 
    generation of hazardous or nonhazardous waste is expected, except 
    for a 3 to 5% increase in sediment removed from the cooling tower. 
    Nor is any change expected in the load on the sewage treatment 
    plant. River water use will remain within the existing agreement 
    with the Susquehanna River Basi[n] Commission. PP&L has determined 
    that power uprate is not an ``unreviewed environmental question.''
        The proposed power uprate therefore requires no change to the 
    ``Environmental Protection Plans'' since it does not involve:
        (a) A significant increase in any adverse environmental impact 
    previously evaluated in the ``Environmental Report--Operating 
    License Stage,'' or the ``Final Environmental Statement,'' or in any 
    decision of the Atomic Safety and Licensing Board;
        (b) A significant change in effluents or power levels, or
        (c) A matter not previously reviewed and evaluated in the 
    documents specified in paragraph (a) which might have a significant 
    adverse environmental impact.
    
    Radiological Environmental Assessment
    
        As discussed previously, the licensee addressed potential 
    radiological impacts attributable to operation at uprated power 
    conditions in Sections 8, 9, and 11 of the initial Topical Report. The 
    licensee concluded:
    
        Adequate margin also exists for the proposed power uprate 
    without exceeding regulatory limits for radiological effects. 
    Current operating experience indicates that actual releases and 
    waste disposal after power uprate will continue to be significantly 
    less than the original estimates. For these reasons, power uprate is 
    not expected to have an adverse effect on the routine operation 
    ``dose commitment'' estimated by previous radiological environmental 
    analyses, and no revision of these analyses is required.
        The environmental assessment includes an estimate of potential 
    exposure from all accident types combined. Regulatory Guide 1.49 
    requires calculation of accident doses at 102% of uprated thermal 
    power, or 3510 MWt. Although direct comparison with the original 
    analyses is not meaningful because of changes in methodology, a 
    comparison on a consistent basis would show that the expected dose 
    is approximately proportional to power. The original calculation was 
    done at 3439 MWt. The estimated potential exposure from all accident 
    types combined will therefore change by about the ratio of 3510/
    3439, or about 2 percent, which is not a significant change compared 
    to the uncertainty in the probability estimates. No revision of 
    these analyses is therefore required.
        (Liquid radwaste throughput may increase up to 5% to a level 
    which is within the processing capability of the system.) The 
    activity levels of some radwaste streams containing coolant 
    activation products may increase up to 10%, due to the 4.5% core 
    flux increase and a 5% crud increase to the reactor which are 
    assumed to occur.
        Since the power uprate level of 3441 MWt is not significantly 
    different from that analyzed previously, it is not anticipated there 
    will be a significant increase in radiological effluents. Also, pre-
    power uprate technical specification limits will be maintained.
    
        The NRC staff has concluded that the NRC's FES (NUREG-0564) is 
    valid for operation at the proposed uprated power conditions. The staff 
    also concluded that the plant operating parameters impacted by the 
    proposed power uprate would remain within the bounding conditions on 
    which the conclusions of the FES are based.
        The NRS staff has reviewed the licensee's re-evaluation of the 
    potential radiological and non-radiological environmental impacts for 
    the proposed action. On the basis of this review, the NRC staff finds 
    that the radiological and non-radiological environmental impacts 
    associated with the proposed small increase in power are essentially 
    immeasurable and do not change the conclusion in the FES that the 
    operation of Susquehanna would cause no significant adverse impact upon 
    the quality of the human environment.
        Accordingly, the Commission concludes that this proposed action 
    would result in no significant radiological or non-radiological 
    environmental impact.
    
    Alternatives to the Proposed Action
    
        Since the Commission concluded that there are no significant 
    environmental effects that would result from the proposed license 
    amendment, any alternative with equal or greater environmental impacts 
    need not be evaluated.
        The principal alternative would be to deny the requested amendment. 
    This would not significantly reduce the environmental impact of plant 
    operation but would restrict operation of Susquehanna, Unit 2 to the 
    currently licensed power level and prevent the facility from generating 
    the approximately 50 MWe that is obtainable from the existing plant 
    design.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the ``Final Environmental Statement related to 
    the operation of Susquehanna Steam Electric Station, Units 1 and 2,'' 
    dated June 1981.
    
    Agencies and Persons Consulted
    
        The Commission's staff reviewed the licensee's request and 
    consulted with the Bureau of Radiation Protection, Pennsylvania 
    Department of Environmental Resources. The State Liaison Officer had no 
    comment regarding the NRC's proposed action.
    
    Finding of No Significant Impact
    
        Based upon the foregoing environmental assessment, the Commission 
    concludes that the proposed action will not have a significant effect 
    on the quality of the human environment. The Commission has determined 
    not to prepare an environmental impact statement for the proposed 
    license amendment.
        For further details with respect to this action, see the 
    application for amendment dated November 24, 1993. This document is 
    available for public inspection at the Commission's Public Document 
    Room, The Gelman Building, 2120 L Street, NW., Washington, DC 20555 and 
    at the Osterhout Free Library, Reference Department, 71 South Franklin 
    Street, Wilkes-Barre, Pennsylvania 18701.
    
        Dated at Rockville, Maryland, this 11th day of March 1994.
    
        For the Nuclear Regulatory Commission.
    Charles L. Miller,
    Dirctor, Project Directorate I-2, Division of Reactor Projects--I/II, 
    Office of Nuclear Reactor Regulation.
    [FR Doc. 94-6412 Filed 3-17-94; 8:45 am]
    BILLING CODE 7590-01-M
    
    
    

Document Information

Published:
03/18/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-6412
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: March 18, 1994, Docket No. 50-388