96-6521. Arizona Public Service Company Palo Verde Nuclear Generating Station, Unit Nos. 1, 2, and 3; Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 61, Number 54 (Tuesday, March 19, 1996)]
    [Notices]
    [Pages 11231-11232]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-6521]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    [Docket Nos. STN 50-528, 50-529, and 50-530]
    
    
    Arizona Public Service Company Palo Verde Nuclear Generating 
    Station, Unit Nos. 1, 2, and 3; Environmental Assessment and Finding of 
    No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of an amendment to Facility Operating License No. 
    NPF-41, NPF-51, and NPF-74 issued to Arizona Public Service Company, 
    (the licensee), for operation of the Palo Verde Nuclear Generating 
    Station, Units 1, 2, and 3, respectively, located in Maricopa County, 
    Arizona.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The Environmental Assessment is written in connection with the 
    proposed core uprate for the Palo Verde Nuclear Generating Station in 
    response to the licensee's application dated January 5, 1996. The 
    proposed action would increase the rated thermal power (RTP) for Palo 
    Verde from the current level of 3800 megawatts thermal (MWt) to 3876 
    MWt, an increase of 2 percent over the current RTP. To support the 
    increased power operation, the licensee has also proposed amendment 
    changes that would lower the allowable reactor coolant system cold-leg 
    temperature limits for all three PVNGS Units and lower the pressurizer 
    safety valve setpoints for Units 1 and 3. The PVNGS Unit 2 safety valve 
    setpoints were revised by Amendment 78, approved March 28, 1995, to the 
    same values being requested for Units 1 and 3. The proposed action is 
    in accordance with the licensee's application for amendment dated 
    January 5, 1996.
    
    The Need for the Proposed Action
    
        The proposed action is needed to increase the electrical output by 
    up to approximately 26 megawatts electric (MWe) and thus provide 
    additional electrical power to the grids which service the commercial 
    and residential areas of the owner utilities (the Salt River Project 
    Agricultural Improvement and Power District, Southern California Edison 
    Company, El Paso Electric Company, Public Service Company of New 
    Mexico, Los Angeles Department of Water and Power, and Southern 
    California Public Power Authority).
    
    Environmental Impacts of the Proposed Action
    
        A 2-percent increase in rated thermal power (RTP) is not a 
    significant increase in power level. The Final Environmental Statement 
    (FES) (NUREG-0841) recognized in the Summary and Conclusions Section 
    that the maximum design thermal output for each unit is 4100 MWt. The 
    proposed increase is less than maximum design thermal output evaluated 
    during the FES construction permit stage (FES-CP). Thus the 
    environmental effects previously evaluated for land and water usage are 
    bounded by those previously evaluated. The increase in RTP does not 
    change any of the conclusions of NUREG-0841.
        The 2-percent RTP increase does not change the method of operation 
    or modify the plant configuration, apart from minor changes in 
    equipment setpoints. Thus no increase in the probability or 
    consequences of an accident is created by the proposed amendment. 
    System and programmatic reviews have been done of the nuclear steam 
    supply system (NSSS) controls, the reactor coolant system, the steam 
    generators, balance-of-plant systems, and the fire protection, 
    equipment qualification, and probability risk assessment programs. The 
    reviews concluded that operation in accordance with the changes 
    proposed in this amendment was acceptable and posed no significant risk 
    to the health and safety of the public. The analysis supporting this 
    amendment demonstrates that the consequences of events under the 
    increased-RTP conditions are within the criteria of the current 
    licensing basis for the PVNGS units. Therefore the amendment, as 
    proposed, does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The increase in RTP does not authorize construction, change the 
    processes, plant equipment, or type of effluents, or significantly 
    affect operation of the units. The proposed amendment will not 
    significantly change the types or amount of radiological effluents from 
    the facility. The changes are within the design basis of the balance-
    of-plant systems, and reviews of the NSSS have demonstrated the 
    acceptability of operation at the increased-RTP conditions. Safety
    
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    analyses of design basis events affected by the increase have been 
    reviewed or reanalyzed and the consequences found to be bounded by 
    current updated final safety analysis report (UFSAR) consequences or 
    within regulatory requirements. In addition, no significant increases 
    in individual or cumulative occupational radiation exposure would 
    result from the proposed changes in operating conditions. Also, the 
    proposed increase in the NSSS power involves no significant change in 
    the amount of any nonradiological impacts associated with operation of 
    the facility, i.e., those previously evaluated and approved in the FES. 
    The Final Environmental Assessment evaluated the environmental impact, 
    assuming the maximum design thermal output of the PVNGS units to be 
    4100 MWt. Thus, the proposed increase in power level is within the 
    scope of the previous reviews performed for the environmental impact of 
    operation of the units. Accordingly, the Commission concludes that 
    there are no significant environmental impacts associated with the 
    proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded that there is no measurable 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impacts need not be 
    evaluated. The principal alternative to the proposed action would be to 
    deny the requested amendment. Denial would not significantly reduce the 
    environmental impact of plant operation and would restrict operation of 
    the PVNGS units to the currently licensed power level, thereby reducing 
    operational flexibility.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the Final Environmental Statement for the Palo 
    Verde Nuclear Generating Station.
    
    Agencies and Persons Consulted
    
        In accordance with NRC policy, on February 28, 1996, the staff 
    consulted with the Arizona State official, Mr. William Wright of the 
    Arizona Radiation Regulatory Agency, regarding the environmental impact 
    of the proposed action. The State official had no comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated January 5, 1996, which is available for public 
    inspection at the Commission's Public Document Room, The Gelman 
    Building, 2120 L Street, NW., Washington, DC, and at the local public 
    document room located at the Phoenix Public Library, 1221 N. Central 
    Avenue, Phoenix, Arizona 85004.
    
        Dated at Rockville, Maryland, this 11th day of March 1996.
    
        For the Nuclear Regulatory Commission.
    Charles R. Thomas,
    Project Manager, Project Directorate IV-2, Division of Reactor Projects 
    III/IV, Office of Nuclear Reactor Regulation.
    [FR Doc. 96-6521 Filed 3-18-96; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Published:
03/19/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-6521
Pages:
11231-11232 (2 pages)
Docket Numbers:
Docket Nos. STN 50-528, 50-529, and 50-530
PDF File:
96-6521.pdf