X94-10302. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 41 (Wednesday, March 2, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-10302]
    
    
    [[Page Unknown]]
    
    [Federal Register: March 2, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
     
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from February 5, 1994, through February 17, 1994. 
    The last biweekly notice was published on February 16, 1994 (59 FR 
    7685).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room P-223, Phillips Building, 7920 Norfolk Avenue, 
    Bethesda, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies 
    of written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By April 1, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, Unit 
    Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendment requests: January 13, 1994
        Description of amendment requests: Request for NRC consent to the 
    indirect transfer of control of El Paso Electric Company's interest in 
    Operating License Nos. NPF-41, NPF-51, NPF-74 and to amend Operating 
    License Nos. NPF-51 and NPF-74 to delete provisions for El Paso 
    Electric Company's sale-leaseback arrangements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis about the issue of no significant hazards 
    consideration, which is presented below:
        Standard 1 -- Involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        This amendment request does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because the proposed change is administrative in nature. 
    The proposed change deletes Sections 2.B.(7)(a) and (b) of License 
    No. NPF-51, and Sections 2.B.(6)(a) and (b) of License No. No. NPF-
    74. These section describe the structure of the financing of El 
    Paso's interest in Palo Verde, specifically authorizing sale and 
    leaseback transactions. The proposed change does not affect the 
    assumptions used in the accident analyses, nor does the proposed 
    change result in changes to the physical configuration of the 
    facility, design parameters, technical specifications, or operation 
    and maintenance of the facility. Therefore, this amendment request 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Standard 2 -- Create the possibility of a new or different kind 
    of accident from any accident previously analyzed.
        This amendment request does not create the possibility of a new 
    or different kind of accident from any accident previously analyzed 
    because the proposed change is administrative in nature. The 
    proposed change deletes Sections 2.B.(7)(a) and (b) of License No. 
    NPF-51, and Sections 2.B.(6)(a) and (b) of License No. NPF-74. These 
    sections describe the structure of the financing of El Paso's 
    interest in Palo Verde, specifically authorizing sale and leaseback 
    transactions. The proposed change does not involve modifications to 
    any of the existing equipment nor does the change affect the 
    operation and maintenance of the facility. Therefore, this amendment 
    request does not create the possibility of a new or different kind 
    of accident not previously analyzed.
        Standard 3 -- Involve a significant reduction in a margin of 
    safety.
        This amendment request does not involve a significant reduction 
    in a margin of safety because it is administrative in nature. The 
    proposed change deletes Sections 2.B.(7)(a) and (b) of License No. 
    NPF-51, and Sections 2.B.(6)(a) and (b) of License No. NPF-74. These 
    sections describe the structure of the financing of El Paso's 
    interest in Palo Verde, specifically authorizing sale and leaseback 
    transactions. The proposed change does not involve changes to any 
    existing plant equipment or accident analyses that provide for or 
    establish margins of safety. There are no changes to the operation 
    or maintenance of the facility and the existing margins of safety 
    are not changed by the proposed change. Therefore, this amendment 
    request does not involve a signigicant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensees' analysis and, based on 
    that review, it appears that the proposed license amendment reflects 
    only a change in the structure of the financing of El Paso's interest 
    in Palo Verde and the three standards of 50.92(c) are satisfied. 
    Therefore, the NRC staff proposes to determine that the amendment 
    requests involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004 Attorney for licensees: 
    Nancy C. Loftin, Esq., Corporate Secretary and Counsel, Arizona Public 
    Service Company, P.O. Box 53999, Mail Station 9068, Phoenix, Arizona 
    85072-3999
        NRC Project Director: Theodore R. Quay
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: February 4, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 3/4.6.4, Containment Systems Combustible 
    Gas Control, by eliminating the 12-hour channel check surveillance 
    requirement for the containment hydrogen monitoring system in 
    conformance with the new Standard Technical Specifications, NUREG-1431.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Final Safety Analysis Report [FSAR] section 6.2.5.2.3 states 
    that the Hydrogen Analyzer is only required to be functioning 
    (continuously indicating and recording hydrogen concentration) 
    within 30 minutes of safety injection initiation. The performance of 
    an analog operational test every 31 days and a channel calibration 
    test every 92 days verifies this operability. Based on this, the 
    monitors will be fully capable of performing their intended design 
    function following a safety injection initiation. Therefore, the 
    elimination of the 12-hour channel check would not increase the 
    probability or consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The Hydrogen Monitors perform an ``indication'' function only, 
    [sic] to help ensure that hydrogen concentrations within containment 
    are maintained below flammable limits during a post-LOCA [loss-of-
    coolant accident] condition. The proposed changes do not involve any 
    modifications or additions to plant equipment and the design and 
    operation of the plant will not be affected. Therefore, the 
    elimination of the 12-hour channel check does not affect any 
    parameters which relate to the margin of safety as defined in the 
    Technical Specifications or the FSAR. Therefore, the proposed 
    changes do not involve a significant reduction in a margin of 
    safety.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed elimination of the 12-hour channel check does not 
    affect any parameters which relate to the margin of safety as 
    defined in the Technical Specifications or the FSAR. Therefore, the 
    proposed changes do not involve a significant reduction in a margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: S. Singh Bajwa
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of amendment request: March 26, 1993
        Description of amendment request: The proposed amendment would 
    modify trip level settings for the Isolation Condenser and High 
    Pressure Core Injection (HPCI) System Steam lines to more conservative 
    values. In addition, the proposed amendment would revise the Emergency 
    Core Cooling System Low-Low Water Level initiation trip level setting 
    tolerance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        HPCI Steamline High Flow Isolation Trip Level Setting
        The purpose of the HPCI leak detection systems are to detect 
    breaks in the system piping. Normal steam flows within the system 
    can fluctuate in excess of 250% rated flow and exceed 500% rated 
    steam flow after experiencing a break. During the original licensing 
    of the plant, it was analytically determined by GE that three times 
    maximum steam flow (300%) is the optimum setpoint for the isolation 
    of HPCI. A 300% steam flow setpoint ensures that spurious trips are 
    avoided and that breaks in the piping are identified. Because the 
    HPCI High Steamline Flow Isolation setpoint is not assumed as an 
    accident precursor, the probability of any previously evaluated 
    accident is not increased by the changed setpoint.
        The proposed changes to the setpoint allow a more accurate and 
    conservative value for 300% steam flow. The proposed change in 
    conjunction with a more conservative field setting ensures HPCI 
    isolation occurring between the range of 300% and 500% steam flow, 
    thus ensuring HPCI isolation in the event of a pipe break. Because 
    the HPCI high steamline flow setpoint will be maintained above 
    normally found operational values (272% steam flow) and below 
    expected conditions with a pipe break (500% steam flow), the 
    consequences of any previously evaluated accident are not increased 
    with the proposed setpoint change.
        solation Condenser Steamline High Flow Isolation Trip Level 
    Setting
        The purpose of the Isolation Condenser leak detection 
    instrumentation is to detect breaks in the system piping. Normal 
    steam flows within the system can fluctuate in excess of 250% rated 
    flow and exceed 500% rated steam flow after experiencing a break. 
    During the original licensing of the plant, it was analytically 
    determined by GE that three times rated steam flow (300%) is the 
    optimum setpoint for the isolation of the Isolation Condenser. A 
    300% steam flow Isolation setpoint ensures that spurious trips are 
    avoided and that breaks in the piping are identified. Because the 
    Isolation Condenser High Steamline Flow setpoint is not assumed as 
    an accident precursor, the probability of any previously evaluated 
    accident is not increased by the changed setpoint. The proposed 
    changes to the setpoint provide a more accurate and conservative 
    field setting for 300% steam flow.
        The proposed changes in conjunction with a more conservative 
    field setting results in Isolation Condenser isolation occurring 
    between the range of 300% and 500% steam flow, thus ensuring 
    Isolation Condenser isolation in the event of a pipe break. Because 
    the Isolation Condenser High Steamline Flow Isolation setpoint will 
    be maintained above normally found operational values (272% steam 
    flow) and below expected conditions with a pipe break (500% steam 
    flow), the consequences of any previously evaluated accident are not 
    increased with the proposed setpoint change.
        Reactor Low-Low Water Level Trip Level Setting Tolerance
        The Low-Low Reactor Water Level trip setting is designed to 
    initiate ECCS when reactor water level is less than or equal to 444 
    inches above vessel zero. Top of active fuel (TAF) is defined as 360 
    inches above vessel zero. -59 inches is 84 inches above TAF. The 
    present trip setting tolerance (84 inches, + 4, - 0, above TAF) only 
    allows a deviation of 4 inches in the conservative direction. The 
    proposed change (greater than or equal to 84 inches) does not impose 
    a restriction on the limit toward the conservative direction. 
    Because a level switch trip level setting by itself is not assumed 
    as an accident precursor, the probability of any previously 
    evaluated accident is not increased by the changed setpoint.
        The proposed change eliminates a restriction on the trip level 
    setting for Low-Low Reactor Water Level. Dresden proposes modifying 
    the acceptance limit of the Low-Low trip setting such that the 
    instrument field setting will not deviate below 84 inches. 
    Therefore, the actuation of appropriate ECCS are unchanged and the 
    consequences of any previously evaluated accident are not increased 
    with the proposed setpoint change.
        Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        HPCI Steamline High Flow Isolation Trip Level Setting
        The purpose of the HPCI Steamline High Flow Isolation trip level 
    setting is to detect breaks in system piping and initiate isolation 
    of the system if breaks are discovered. Normal steam flows within 
    the system can fluctuate as high as 250% rated flow and exceed 500% 
    rated steam flow after experiencing a break. 300% steam flow has 
    been used as the setpoint to ensure that spurious trips are avoided 
    and that breaks in the piping are identified. The changes to the 
    HPCI High Steamline Flow setpoint ensure that isolation occurs at 
    300% rated steam flow (below 500% rated steam flow). The current 
    setpoint will also isolate below 500% rated steam flow. Because the 
    new setpoint continues to allow normal operational flexibility and 
    ensures isolation in the event of a pipe break, the proposed changes 
    do not create the possibility of a new or different kind of accident 
    than previously evaluated.
        Isolation Condenser Steamline High Flow Isolation Trip Level 
    Setting
        The purpose of the Isolation Condenser Steamline High Flow 
    Isolation trip level setting is to detect breaks in system piping 
    and initiate isolation of the system if breaks are discovered. 
    Normal steam flows within the system can fluctuate in excess of 250% 
    rated flow and exceed 500% rated steam flow after experiencing a 
    break. 300% steam flow has been used as the setpoint to ensure that 
    spurious trips are avoided and ensures that isolation occurs at 300% 
    rated steam flow (below 500% rated steam flow). The current setpoint 
    will also isolate below 500% rated steam flow. Because the new 
    setpoint continues to allow normal operational flexibility and 
    ensures isolation in the event of a pipe break, the proposed changes 
    do not create the possibility of a new or different kind of accident 
    than previously evaluated.
        Reactor Low-Low Level Trip Level Setting Tolerance
        The Reactor Low-Low Water Level trip setting is designed to 
    initiate the appropriate ECCS when Reactor Water Level is 
    decreasing. The proposed change to the setpoint only eliminates the 
    overly burdensome restriction within the setpoint tolerances. The 
    absolute low limit of 84 inches is unchanged, thus maintaining all 
    assumptions related to 84 inches (-59 inches indicated level) within 
    Dresden's Safety Analysis. The removal of the upper tolerance will 
    not increase the probability of inadvertent ECCS initiation since 
    the actual field setting will be at a reactor vessel level which has 
    not been reached in 40 + years of operation at Dresden Units 2 and 
    3. Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident than previously evaluated.
        Involve a significant reduction in the margin of safety because:
        High Pressure Coolant Injection Setpoint
        The HPCI high steamline flow setpoint ensures that isolation 
    occurs at 300% maximum steam flow (below 500% rated steam flow). The 
    current Technical Specification setpoint will also allow isolation 
    below 500% rated steam flow but at a value greater than 300%. Thus, 
    the proposed setpoint isolates at a lower steam flow rate than the 
    current limit. Therefore, because isolation of HPCI would occur at a 
    lower steam flow rate during a pipe break, the proposed changes do 
    not involve a significant reduction in the margin of safety.
        Isolation Condenser Steamline High Flow Isolation Trip Level 
    Setting
        The Isolation Condenser High Steamline Flow Isolation Trip Level 
    setting ensures that isolation occurs at 300% rated steam flow 
    (below 500% rated steam flow). The current setpoint will also 
    isolate below 500% rated steam flow but at a value greater than 
    300%. Thus, the proposed setpoint isolates at a lower steam flow 
    rate than the current limit. Therefore, because isolation of the 
    Isolation Condenser would occur at a lower steam flow rate during a 
    pipe break, the proposed changes do not involve a significant 
    reduction in the margin of safety.
        Reactor Low-Low Level Trip Level Setting Tolerance
        The Reactor Low-Low Water Level trip setting tolerance ensures 
    the proper initiation of appropriate ECCS in the event of a loss of 
    inventory to the vessel. The proposed change to the setpoint only 
    eliminates the restriction within the setpoint tolerances. The 
    absolute low limit of 84 inches is unchanged, thus maintaining all 
    assumptions related to 84 inches (minus 59 inches indicated) within 
    Dresden's Safety Analysis. Therefore, the proposed changes do not 
    involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Morris Public Library, 604 
    Liberty Street, Morris, Illinois 60450
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: James E. Dyer
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad 
    Cities Nuclear Power Station, Units 1 and 2, Rock Island County, 
    Illinois
    
        Date of amendment request: December 20, 1993
        Description of amendment request: The proposed amendment would 
    revise a minimum critical power ratio (MCPR) safety limit from 1.06 to 
    1.07 based on General Electric Standard Application for Reactor Fuel II 
    (GESTAR II) NEDE-24011-P-A-10 for GE10 fuel design. The NRC staff has 
    previously reviewed and approved the GE10 fuel design.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because:
        The change is based on GE's generic rule licensing document 
    GESTAR II (NEDE-24011-P-A-10) which has conservatively addressed the 
    use of GE10 fuel in D-lattice cores with NRC approved methods and 
    therefore does not adversely affect the consequences of previously 
    evaluated accidents. The Safety Limit MCPR change does not affect 
    the probability of analyzed accidents because it does not adversely 
    impact any equipment important to safety. Increasing the Safety 
    Limit MCPR from 1.06 to 1.07 upon implementation of GE10 fuel for 
    Cycle 14 operation of Quad Cities Units 1 and 2 therefore does not 
    involve a significant increase in the probability or consequences of 
    any accident previously evaluated in the FSAR.
        The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    because:
        The Safety Limit MCPR change results from the use of NRC 
    approved methods in GESTAR II NEDE-24011-P-A-10 for application to 
    GE10 fuel for Cycle 14 for Quad Cities Units 1 and 2. The Safety 
    Limit MCPR change does not result in any new interaction with 
    equipment related to the safe shutdown of the plant. The change does 
    not adversely impact equipment important to safety and, therefore 
    does not create the possibility of a new or different kind of 
    accident scenario. Therefore, the Safety Limit MCPR change from 1.06 
    to 1.07 in no way creates the possibility of a new or different kind 
    of accident scenario from any accident previously evaluated.
        The proposed change does not involve a significant reduction in 
    a margin of safety because:
        Since the GE10 design in a D-lattice core has a geometry between 
    C-lattice and D-lattice designs and the C-lattice design has a 
    higher, more restrictive safety limit MCPR that the D-lattice 
    design, the use of C-lattice safety limit MCPR for the GE10 design 
    is a conservative approach. The GE10 fuel design has been 
    generically analyzed with approved methods per GESTAR II NEDE-24011-
    P-A-10 and the use of the 1.07 Safety Limit MCPR value has been 
    previously approved as conservative for application to GE10 fuel in 
    D-lattice plants such as Quad Cities. Therefore, the proposed change 
    to increase the Safety Limit MCPR from 1.06 to 1.07 maintains the 
    margin to safety relative to the current level.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: James E. Dyer
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: December 10, 1993
        Description of amendment request: The proposed amendment request 
    would revise the Technical Specifications to amend (1) Section 5.3.A 
    (Reactor Core) to allow the use of VANTAGE + fuel with ZIRLO cladding 
    and fuel with filler rods to allow fuel reconstitution, and (2) the 
    Basis to Section 2.1 (Safety Limit: Reactor Core) to allow the use of 
    departure from nucleate boiling (DNB) Correlations applicable to 
    VANTAGE + fuel.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Consistent with the requirements of 10 CFR 50.92, the enclosed 
    application involves no significant hazards based on the following 
    information:
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response:
        Neither the probability nor the consequences of an accident 
    previously analyzed is increased due to the proposed changes. As 
    discussed in [Letter from Thadani to Tritch, ``Acceptance
    
        for Referencing of Topical Report WCAP-12610, VANTAGE + Fuel 
    Assembly Reference Core Report'' (TAC No. 77258) July 1, 1991] the 
    fuel containing ZIRLO clad will meet all the same material and 
    mechanical design criteria as the Zircaloy clad fuel. The use of 
    approved Westinghouse Methodology for fuel assembly reconstitution 
    as documented in [Letter from Thadani to Tritch, ``Acceptance for 
    Referencing of Topical Report WCAP-13060-P, Westinghouse Fuel 
    Assembly Reconstitution Evaluation Methodology'' (TAC No. M821391), 
    March 30, 1993] will ensure that all criteria are met. The change to 
    the basis of Section 2.1 more accurately describes DNB methodology 
    and application.
        2. Does the proposed license amendment create the possibility of 
    a new or different kind of accident from any previously evaluated?
        Response:
    
        The changes will not create the possibility of a new or 
    different kind of accident. The proposed changes involve approved 
    methodology which have been shown to meet design and safety 
    criteria. In addition, approved procedures will be used to implement 
    the changes.
        Response:
        3. Does the proposed amendment involve a significant reduction 
    in the margin of safety?
        The proposed amendment does not involve a significant reduction 
    in the margin of safety. The changes involve the use of approved 
    methodology which meet design and safety criteria. The change to the 
    Section 2.1 basis is descriptive and will more accurately describe 
    the DNB methodology used in conjunction with the use of VANTAGE + 
    fuel.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: Robert A. Capra
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: September 28, 1993
        Description of amendment request: The requested amendments would 
    delete the portion of the 18-month surveillance requirement on the 
    autoclosure interlock (ACI) contained in TS 4.5.2.d associated with 
    verifying that the decay heat removal system suction isolation valves 
    automatically close on a reactor coolant system pressure signal. The 
    terms decay heat removal (ND) and residual heat removal (RHR) are used 
    interchangeably here. Also, an obsolete footnote to TS 4.5.2.e relating 
    to the completion of the first Unit 1 refueling outage is proposed to 
    be deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The requested amendments reference Westinghouse topical report 
    WCAP-11736-A, ``Residual Heat Removal System Autoclosure Interlock 
    Removal Report for the Westinghouse Owners Group'', for the general 
    justification and safety analysis for removing the ACI feature from 
    the Catawba ND suction isolation valves. This WCAP, which 
    specifically covers the Catawba Nuclear station, has been deemed an 
    acceptable reference by the NRC for use in making plant-specific 
    licensing submittals. Additional Catawba-specific information/ 
    improvements and analyses, as required by the WCAP and associated 
    NRC safety evaluation, have been either completed or committed to, 
    thereby ensuring that the WCAP/SE conclusion that removal of the RHR 
    ACI produces a net safety benefit remains valid.
        Criterion 1
        The requested amendments will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The deletion of the RHR ACI was analyzed in the WCAP for 
    Callaway Nuclear Station in terms of (1) the frequency of an 
    interfacing LOCA, (2) the availability of the RHR system, and (3) 
    the effect on overpressure transients. Callaway is the WCAP's 
    reference plant for Catawba Units 1 and 2, and a Catawba-specific 
    Probabilistic Risk Assessment (PRA) review of the WCAP determined 
    that removal of the ND ACI at Catawba will not invalidate the basic 
    conclusions of the WCAP. Consequently, the following information 
    from the Callaway analysis is considered applicable to Catawba Units 
    1 and 2.
        With the removal of the ACI and addition of a control room 
    alarm, the probabilistic risk analysis predicts a decrease in the 
    frequency of interfacing LOCAs from 1.52E-06/year to 1.16E-06/year, 
    a decrease of approximately 24%.
        The availability of the RHR system was analyzed in three phases: 
    initiation, short term cooling, and long term cooling. The 
    probabilistic analysis indicated that deletion of the RHR ACI has no 
    impact on the failure probability for RHR initiation. During short 
    term cooling (72 hours after initiation), RHR ACI deletion decreased 
    the RHR failure probability by 12%, from 1.64E-02 to 1.44E-02. The 
    long term cooling RHR failure probability was calculated to decrease 
    by 70%, from 3.91E-02 to 1.17E-02.
        Appendix D of the WCAP presents the analysis used to determine 
    the effect of removal of the ACI on overpressurization transients. 
    The analysis categorizes the types of initiating events, determines 
    their frequency of occurrence, and then identifies the consequences 
    of these occurrences both with and without the ACI feature. The 
    result is a list of overpressure consequence categories with 
    associated failure probabilities (reference the WCAP's Appendix D, 
    Tables D-14, -15, and -16). For the charging/safety injection event, 
    consequence frequencies increased on the order of 1.0E-12/shutdown 
    year. This is an insignificant increase, as the overall consequence 
    frequency of the charging/safety injection event is 1.25E-01. 
    Likewise, for the letdown isolation with RHR system operable case, 
    one frequency category was increased on the order of 1.0E-15. Again, 
    this is insignificant when compared with the total frequency of 
    these events of 1.25E-01. For the letdown isolation with RHR system 
    isolated event, the overall consequence frequency was reduced from 
    4.45E-01 to 2.22E-01. This occurs because many spurious closures of 
    the RHR isolation valves cause the isolation of letdown. Removing 
    the RHR ACI reduces the frequency of this event by approximately 
    50%. It is concluded that the removal of the RHR ACI circuitry has 
    an insignificant impact on the frequency of overpressurization 
    events at Callaway (and thus Catawba) Nuclear Station.
        Criterion 2
        The requested amendments will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The effect of an overpressure transient at cold shutdown 
    conditions will not be altered by removal of the ND ACI function. 
    With or without the ACI function, the ND system could be subject to 
    overpressrue for which the ND relief valves must be relied upon to 
    limit pressure to within ND design parameters. While it is true that 
    the ACI initiates an automatic closure of the ND suction/isolation 
    valves on high NC system pressure, overpressure protection of the ND 
    system is provided by the ND system relief valves and not by the 
    suction/isolation valves that isolate the ND system from the NC 
    system. (Refer to NUREG-0954, ``Safety Evaluation Report related to 
    the operation of Catawba Nuclear Station, Units 1 and 2,'' Section 
    5.4.4.3.)
        The purpose of the ACI feature is to ensure that there is a 
    double barrier between the ND system and the NC system when the 
    plant is at normal operating conditions (i.e., heated and 
    pressurized) and not in the ND cooling mode. Thus, the ACI feature 
    serves to preclude conditions that could lead to a LOCA outside of 
    containment due to operator error. The safety function of the ACI is 
    not to isolate the ND system from the NC system when the ND system 
    is operating in the decay heat removal mode.
        There are several methods to ensure that there is a double 
    barrier between the ND system and the NC system when the plant is at 
    normal operating conditions. First, plant operating procedures 
    instruct the operators to isolate the ND system during plant heatup. 
    Second, the alarm that will be installed as part of this change will 
    annunciate in the control room given an open or intermediate valve 
    position signal in conjunction with a high NC pressure signal. This 
    alarm will alert operators that any of the four suction/isolation 
    valves is (are) not fully closed and that double isolation has not 
    been achieved. In conjunction with this alarm, operators will be 
    trained using an annunciator response procedure to ensure that they 
    act to restore double isolation or return to a safe shutdown 
    condition. Third, the Open Permissive Interlock (OPI), which is not 
    being removed, will prevent the opening of the valves whenever NC 
    system pressure is greater than 385.5 psig.
        Since relief valves prevent overpressurization of the ND system 
    during shutdown conditions and since several methods are in place to 
    ensure that the ND system is isolated from the NC system during 
    normal plant conditions, removal of the ACI will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Criterion 3
        The requested amendments will not involve a significant 
    reduction in a margin of safety. The ND ACI function is not a 
    consideration in a margin of safety in the basis for any technical 
    specification. Since the probabilistic analysis of the WCAP for 
    Callaway (which is applicable to Catawba as discussed above) 
    indicates that the availability of the RHR system is increased with 
    the removal of the ACI, overall safety will be increased.
        In addition, similar amendments for other Westinghouse plants in 
    the past have been determined to not involve significant hazards 
    considerations.
        Based upon the preceding analyses, Duke Power Company concludes 
    that the requested amendments do not involve a significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Loren R. Plisco, Acting
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: January 27, 1994
        Description of amendment request: The requested amendments delete 
    the verification that each upper and lower Containment Purge System 
    (VP) supply and exhaust valve actuates to its isolation position on a 
    High Relative Humidity (70%) isolation test signal and will 
    allow elimination of the humidity control function of the VP System 
    humidistats.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        CRITERION 1
        This TS [Technical Specification] amendment will not increase 
    the probability or consequences of an accident which has been 
    previously evaluated. No physical changes will be made to the plant 
    that would impact fuel handling inside containment, therefore, there 
    is no increase in the probability of an accident. Control wiring 
    changes that remove the humidistats from the [Containment Purge] 
    System control circuits will be the only physical change.
        The heaters will be maintained providing additional margin over 
    analyzed conditions. For the reasons stated above, there will be no 
    increase in the consequences of an accident previously evaluated.
        CRITERION 2
        This proposed TS amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. This proposed TS amendment will not cause any physical 
    changes to the plant that will impact the handling of fuel inside 
    containment or changes to fuel handling procedures. Because the 
    plant will operate the same way it does now, this proposed amendment 
    does not create the possibility of any new or different accident 
    from any previously evaluated.
        CRITERION 3
        This proposed TS change will not cause a significant reduction 
    in the margin of safety. The test method use[d] to evaluate the 
    carbon after TS changes 90 ([Unit] 1) and 84 
    ([Unit] 2) does not consider heater availability. However the 
    heaters will be tested and maintained per Technical specification 
    4.9.4.2.d.2. Therefore, the relative humidity of the air entering 
    the carbon adsorber is never expected to reach 95% [relative 
    humidity].
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Loren R. Plisco, Acting
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, 
    Unit No. 1 (ANO-1), Pope County, Arkansas
    
        Date of amendment request: January 13, 1994
        Description of amendment request: This amendment revises the 
    specifications governing the reactor protection (RPS). It modifies the 
    use of the RPS channel bypass as specified by Technical Specification 
    (TS) 3.5.1.3 and revises a note with Table 3.5.1-1, to refer to a more 
    appropriate action.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The RPS and EFIC [emergency feedwater initiation and control] 
    system provide accident mitigation features and are not considered 
    to be accident initiators. The accident mitigation features of the 
    plant are not affected by the proposed amendment. In any 
    configuration allowed by the revised specifications, the trip logic 
    instituted on the RPS is at least equivalent to the trip logic 
    instituted by placing a channel in channel or maintenance bypass. 
    The RPS remains single-failure proof with one channel in channel 
    bypass, manually tripped, or with an inoperable function unbypassed 
    in the untripped state. Therefore, upon receipt of an initiating 
    signal, a single failure will not prevent the proper actuation of 
    RPS. Should a channel of RPS contain an inoperable function 
    unbypassed in the untripped condition which does not affect an EFIC 
    channel, any channel of EFIC may be placed in maintenance bypass. 
    RPS and EFIC remain single-failure proof in this configuration.
        Administrative controls are established to ensure that all 
    inoperable RPS functions are evaluated for continued operation in 
    the untripped state. Upon detection of a failed function in any 
    channel of RPS, the administratively controlled condition reporting 
    process evaluates the failure and its effect on other systems for 
    continued operability. The operator is informed of the continuing 
    status of inoperable functions through the use of Station Log 
    entries and Plant Status board entries. In addition, during 
    operation with an inoperable function in the untripped, unbypassed 
    condition, the remaining RPS channel key-lock channel bypass 
    switches will be ``Hold Carded'' (tagged) to prevent their operation 
    without prior management approval consistent with the requirements 
    of TS Table 3.5.1-1. Plant management maintains the responsibility 
    to approve continued operation with inoperable functions unbypassed 
    in the untripped state to ensure that the plant is operated in the 
    safest configuration with regard to the extent of the failure, and 
    the plant operating conditions. Prior to placing any channel of RPS 
    or EFIC in bypass, the operator checks the status of redundant 
    systems for operability and TS compliance and takes the proper 
    action as required by existing plant conditions, plant operating 
    procedures and TS.
        The clarification to TS 3.5.1.3 which directs the operator to 
    the appropriate actions if multiple channels become inoperable, or 
    in the event of an inoperable channel or inoperable function 
    occurring concurrent with one channel in bypass is considered to be 
    administrative in nature. The change to Note 6 of Table 3.5.1-1 
    results in the correction of misleading information and directs the 
    Operator to place the plant in a safe mode depending on the system 
    which is affected by a failure, and is also considered to be 
    administrative in nature. The Bases changes add additional 
    information to clarify the specifications.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The probability or consequences of equipment important to safety 
    malfunctioning will not be increased. In any configuration allowed 
    by the revised specifications, the trip logic instituted on the RPS 
    is at least equivalent to the trip logic instituted by placing a 
    channel in channel bypass. The RPS remains single-failure proof with 
    one channel in channel bypass, manually tripped, or with an 
    inoperable function unbypassed in the untripped state. Therefore, 
    upon receipt of an initiating signal, a single failure will not 
    prevent the proper actuation of RPS. Should a channel of RPS contain 
    an inoperable function unbypassed in the untripped condition which 
    does not affect an EFIC channel, any channel of EFIC may be placed 
    in maintenance bypass. RPS and EFIC remain single-failure proof in 
    this configuration.
        The clarification to TS 3.5.1.3 which directs the operator to 
    the appropriate actions if multiple channels become inoperable, or 
    in the event of an inoperable channel or inoperable function 
    occurring concurrent with one channel in bypass is considered to be 
    administrative in nature. The change to Note 6 of Table 3.5.1-1 is 
    also considered to be administrative in nature, in that misleading 
    information in the specification has been corrected to an 
    appropriate requirement. The Bases changes add additional 
    information to clarify the specifications.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The RPS and EFIC system have the same capabilities to mitigate 
    and/or prevent accidents as they had prior to this proposed change. 
    Allowing flexibility in the response to a function failure in one 
    channel of RPS allows placing the plant in the safest operating 
    condition for the existing plant conditions considering the extent 
    of the function failure. Operation of an RPS channel with an 
    inoperable function unbypassed in the untripped state results in 
    placing the inoperable function in a 2-out-of-3 trip logic 
    (equivalent to channel bypass) while the remainder of the RPS 
    functions remain in the normal 2-out-of-4 trip logic. The ANO-1 RPS 
    has been reviewed as a 3 channel system with one channel in bypass. 
    Implementing this change results in additional conservatism with 
    respect to any postulated single-failures.
        Administrative controls are established to ensure that all 
    inoperable RPS functions are evaluated for continued operation in 
    the untripped state. Upon detection of a failed function in any 
    channel of RPS, the administratively controlled condition reporting 
    process evaluates the failure and its effect on other systems for 
    continued operability. The operator is informed of the continuing 
    status of inoperable functions through the use of Station Log 
    entries and Plant Status board entries. In addition, during 
    operation with an inoperable function in the untripped, bypassed 
    condition, the remaining RPS channel key-lock channel bypass 
    switches will be ``Hold Carded'' (tagged) to prevent their operation 
    without prior management approval consistent with the requirements 
    of TS Table 3.5.1-1. Plant management maintains the responsibility 
    to approve continued operation with inoperable functions unbypassed 
    in the untripped state to ensure that the plant is operated in the 
    safest configuration with regard to the extent of the failure, and 
    the plant operating conditions. Prior to placing any channel of RPS 
    or EFIC in bypass, the operator checks the status of redundant 
    systems for operability and TS compliance and takes the proper 
    action as required by existing plant conditions, plant operating 
    procedures and TS. Should a channel of RPS contain an inoperable 
    function unbypassed in the untripped condition which does not affect 
    an EFIC channel, any channel of EFIC may be placed in maintenance 
    bypass. RPS and EFIC remain single-failure proof in this 
    configuration.
        The clarification of TS 3.5.1.3 which directs the operator to 
    the appropriate actions if multiple channels become inoperable, or 
    in the event of an inoperable channel or inoperable function 
    occurring concurrent with one channel in bypass is considered to be 
    administrative in nature. The change to Note 6 or Table 3.5.1-1 
    results in the correction of misleading information and directs the 
    Operator to place the plant in a safe mode depending on the system 
    which is affected by a failure, and is also considered to be 
    administrative in nature. The Bases changes add additional 
    information to clarify the specifications.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: January 13, 1994
        Description of amendment request: This amendment requests the 
    removal of the interim technical specification limit on the number of 
    spent fuel assemblies that may be stored in the spent fuel pool at 
    Grand Gulf Nuclear Station.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. No significant increase in the probability or consequences of 
    an accident previously evaluated results from this change.
        The NRC approved the installation of high density spent fuel 
    storage racks in Amendment 17 to the Grand Gulf Nuclear Station 
    (GGNS) Operating License. This amendment also brought GGNS into 
    compliance with Standard Review Plan criteria which required 
    maintaining the spent fuel pool at less than or equal 140 deg.F. The 
    140 deg.F Technical Specifications (TS) limit remains in effect 
    thereby preventing operation at excessive temperatures.
        The only outstanding question from Amendment 17, which resulted 
    in a 2324 assembly technical specification limit, was whether the 
    fuel pool cooling system could handle the heat load of a full fuel 
    pool without excessive reliance on residual heat removal for 
    extensive fuel pool cooling assist. Entergy Operations' proposed 
    solution to this question was accepted in the NRC's letter dated 
    July 30, 1992. The NRC accepted the solution pending submittal of 
    results from tests to verify the specified flows. These results were 
    submitted in a letter dated November 08, 1993.
        With previous approval of the installation of the high density 
    spent fuel storage racks, the confirmation of adequate heat removal 
    capability, and the 140 deg.F TS temperature limit, removal of the 
    2324 limit to allow full use of the spent fuel pool would not cause 
    an increase in the probability or consequences of an accident 
    previously evaluated.
        2. This change would not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The additional heat load generated by a full spent fuel pool 
    (4348 assemblies) was evaluated. The evaluation concluded that full 
    use of the spent fuel pool storage spaces would not exceed the 
    temperature limits as are currently in place with the 2324 limit. 
    The NRC letter dated July 30, 1992 and Entergy Operations letter 
    dated November 08, 1993 resolved all outstanding heat removal 
    questions. Therefore, this change would not create the possibility 
    of a new or different kind of accident from any previously analyzed.
        3. This change would not involve a significant reduction in a 
    margin of safety.
        Entergy Operations demonstrated in their November 01, 1991 
    letter that the fuel pool temperature could be maintained at or 
    below 140*F as specified in TS 3/4.7.9. This letter also 
    demonstrated the ability to handle single active failures. Approval 
    of measures outlined in this letter was provided in a Safety 
    Evaluation Report contained in an NRC letter dated July 30, 1992.
        Given the 140 deg.F maximum temperature requirement as contained 
    in TS 3/4.7.9 and compliance with single active failure criteria, 
    this change would not involve a significant reduction in a margin of 
    safety.
        Based on the above evaluation in accordance with 10CFR50l92(c), 
    Entergy Operations, Inc. has concluded that operation in accordance 
    with the proposed amendment involves no significant hazards 
    considerations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, Post Office Box 1406, S. Commerce at Washington, Natchez, 
    Mississippi 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: December 28, 1993
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications (TS) for Turkey Point Units 3 and 4 
    to incorporate features for steam generator (SG) overfill protection. 
    Specifically, TS Tables 3.3-2, 3.3-3, 4.3-2 and the associated BASES 
    section would be revised to add SG Water Level-High-High protection 
    logic, instrumentation trip setpoints and surveillance requirements. 
    The proposed TS changes would be in accordance with NRC Generic Letter 
    (GL) 89-19, ``Safety Implication of Control Systems in LWR Nuclear 
    Power Plants.''
        Basis for proposed no significant hazards consideration 
    determination: As a result of the technical resolution of USI A-47, 
    ``Safety Implications of Control Systems in LWR Nuclear Power Plants,'' 
    the Nuclear Regulatory Commission (NRC or the staff) concluded that all 
    Pressurized Water Reactors (PWR) plants should provide automatic SG 
    overfill protection. On September 20, 1989, the staff issued GL 89-19 
    and recommended that plant procedures and TS include provisions for 
    automatic SG overfill protection including surveillance requirements to 
    assure that automatic overfill protection is available to mitigate main 
    feedwater overfeed events during reactor power operation.
        The licensee proposed TS changes in response to GL 89-19. No 
    physical changes to the plant would be required as a result of the 
    proposed license amendments.
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Including the SG Overfill protection requirements in the 
    Technical Specifications is not assumed in the initiation of any 
    analyzed event. These amendments will not increase the probability 
    or consequences of an accident previously evaluated since the SG 
    overfill event is not required or assumed for accident mitigation in 
    any Updated Final Safety Analysis Report (UFSAR) safety analyses 
    that comprise Turkey Point licensing basis. The additional 
    requirements for the SG overfill system helps ensure that continuous 
    addition of feedwater and carryover of excessive moisture to the 
    turbine, is prevented. As a result, equipment protection is improved 
    by the availability of this system function. As such, operation of 
    the facility in accordance with the proposed amendments would not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The operation of the facility will not change as a result of the 
    proposed license amendments, since Turkey Point currently maintains 
    this protection logic. This change involves only the inclusion of 
    the systems requirements into the Technical Specifications. The 
    proposed change will not impose any new or unique requirements. 
    Therefore, operation of the facility in accordance with the proposed 
    amendments will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The proposed change does not involve a significant reduction in 
    a margin of safety as the function, operation and testing of the 
    installed SG Overfill protection is not described in the UFSAR. In 
    addition, the SG overfill protection logic is not required or 
    assumed for accident mitigation in any of the safety analyses that 
    comprise the Turkey Point licensing basis. The proposed change 
    formalizes the existing design, operating and testing requirements 
    in the Technical Specifications. Therefore, the proposed change does 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: Harold F. Reis, Esquire, Newman and Holtzer, 
    P.C., 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of amendment request: December 30, 1993
        Description of amendment request: The proposed change would allow a 
    one time extension of the allowable outage time for each residual heat 
    removal (RHR) pump from 3 to 7 days to allow modifications to the RHR 
    system while the plant is in Mode 1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change to the Technical Specifications does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated because the redundant train will 
    remain available to assure that the RHR will respond to an accident 
    as assumed in the accident analysis. A one time increase in the 
    allowable outage time from 3 to 7 days has been shown to have only a 
    small effect on the calculated frequency of core damage.
        2. The proposed change to the Technical Specifications does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated because the change only results in 
    a one time increase of the allowable outage time. It does not result 
    in an operational condition different from that which has already 
    been considered by the Technical Specifications.
        3. The proposed addition to the Technical Specifications does 
    not involve a significant reduction in a margin of safety because 
    the effects of increasing the allowed outage time on the calculated 
    core damage frequency has been evaluated and determined to be small.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308
        NRC Project Director: Loren R. Plisco, Acting
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of amendment request: December 22, 1993
        Description of amendment request: The proposed amendment would make 
    editorial changes to correct typographical and administrative errors in 
    the Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The amendment would only correct 
    administrative and typographical errors. No physical changes to the 
    plant or to the operation of the plant would result from this 
    amendment.
        2) The proposed amendment will not create the possibility of a 
    new or different kind of accident from any evaluated previously. The 
    amendment would only correct administrative and typographical 
    errors. No physical changes to the plant or to operation of the 
    plant would result from this amendment.
        3) The proposed amendment will not reduce the margin of safety. 
    The amendment would only correct administrative and typographical 
    errors. No physical changes to the plant or to operation of the 
    plant would result from this amendment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401
        Attorney for licensee: Jack Newman, Esquire, Kathleen H. Shea, 
    Esquire, Newman and Holtzinger, 1615 L Street, NW., Washington, DC 
    20036
        NRC Project Director: John N. Hannon
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of amendment request: January 21, 1994
        Description of amendment request: The proposed amendment would 
    change the name of the company licensed to own a share of and operate 
    the Duane Arnold Energy Center (DAEC) from Iowa Electric Light and 
    Power Company to IES Utilities Incorporated, wherever it is referenced 
    in the Operating License and Technical Specifications for DAEC. The 
    title of the position responsible for the management of the Nuclear 
    Division has also been changed to ``Vice President, Nuclear'' from 
    ``Manager-Nuclear Division.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. No physical or operational changes to the DAEC 
    will result from changing the corporate name or the position title. 
    The DAEC will continue to be operated in the same manner with the 
    same organization. The position title change results from the 
    elimination of a layer of management. Formerly, the Manager-Nuclear 
    Division reported through the Vice President, Production to the 
    President of IELP. Now the Nuclear Division is headed by the Vice 
    President, Nuclear who reports directly to the President of the 
    corporation.
        2) The proposed amendment does not create the possibility of a 
    new or different kind of accident from any previously evaluated. No 
    physical or operational changes will result. The title change 
    results from the elimination of a layer of management.
        3) The proposed change will not reduce any margin of safety. 
    This change only revises the operating company name and changes a 
    title.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401
        Attorney for licensee: Jack Newman, Esquire, Kathleen H. Shea, 
    Esquire, Newman and Holtzinger, 1615 L Street, NW., Washington, DC 
    20036
        NRC Project Director: John N. Hannon
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of amendment requests: January 17, 1994
        Description of amendment requests: The proposed amendments would 
    change Technical Specification (TS) 3/4.1.3 for both units to increase 
    the limit for control rod misalignment at or below 85% rated thermal 
    power (RTP). The proposed changes would also increase the TS limit for 
    control rod 8misalignment about 85% RTP if there is sufficient margin 
    in the heat flux (FQ(Z)) and the nuclear enthalpy 
    (FNdelta H) hot channel factors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Per 10 CFR 50.92, a proposed amendment to an operating license 
    will not involve a significant hazards consideration if the proposed 
    amendment satisfies the following three criteria:
        1. Does not involve a significant increase in the probability or 
    consequences of an accident previously analyzed,
        2. Does not create the possibility of a new or different kind of 
    accident from any accident previously analyzed or evaluated, or
        3. Does not involve a significant reduction in a margin of 
    safety.
        Criteria 1 and 3
        As seen in Attachment 4 [of the amendment request], sufficient 
    margin exists in power distribution at 85% RTP to allow for 
    increased misalignment. At 100% RTP, increased misalignment is 
    allowed only if there is adequate margin in the peaking factors. 
    Therefore, initial conditions remain unchanged from that assumed in 
    the safety analyses. As far as the dropped rod and rod ejection 
    accidents are concerned, the analyses were performed with 
    conservative assumptions to envelope the increased misalignment. It 
    should be noted that the power dependent insertion limit for Unit 1 
    will be changed in a conservative manner at the beginning of cycle 
    14. Based on these analyses, it is concluded that the proposed T/S 
    changes do not significantly increase the probability or 
    consequences of a previously analyzed accident or constitute a 
    significant reduction in the margin of safety.
        Criterion 2
        The proposed T/S changes will not result in physical changes to 
    the plant. Therefore, we believe that the proposed T/S changes will 
    not create the possibility of a new or different kind of accident 
    from any previously evaluated. Also, operation of the reactor with 
    possible deeper rod insertion will not create the possibility of a 
    new or different kind of accident.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: A. Randolph Blough, Acting
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: January 21, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 4.6.3, (Emergency Power Sources) to 
    eliminate unnecessary testing of an operable emergency diesel generator 
    (EDG) when the redundant EDG becomes inoperable. Eliminating 
    unnecessary testing will potentially increase EDG reliability by 
    reducing the stresses caused by such testing. The licensee stated that 
    this proposed change is consistent with the guidance provided in NUREG-
    1366, ``Improvements to Technical Specifications Surveillance 
    Requirements,'' and NUREG-1433, ``Improved Standard Technical 
    Specifications, General Electric Plants.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Technical Specification 4.6.3.e requires that the operable 
    diesel-generator be manually started and operated at rated load for 
    a minimum time of one hour immediately and once per week thereafter 
    in the event any diesel-generator becomes inoperable.
        Niagara Mohawk proposes to revise Technical Specification 
    4.6.3.e such that if a diesel-generator is declared inoperable due 
    to preplanned maintenance or testing or due to a support system 
    being inoperable, redundant diesel-generator testing would not be 
    required. Declaring a diesel-generator inoperable due to preplanned 
    maintenance or testing or due to a support system being inoperable 
    does not affect the reliability of the operable diesel-generator nor 
    does it in any way imply that a common cause failure exists.
        The normally required Technical Specification surveillance 
    testing schedule demonstrates acceptable reliability and assures 
    that the operable diesel-generator is capable of performing its 
    intended safety function.
        Niagara Mohawk proposes to add wording to Technical 
    Specification 4.6.3.e to permit an operator to evaluate a diesel-
    generator failure to determine if a common cause failure exists 
    before requiring testing of the redundant diesel-generator. As noted 
    above, the intent of the additional diesel-generator testing is, in 
    part, to determine if a common cause failure exists. Once the 
    potential for a common cause failure has been examined and 
    dismissed, testing beyond the normal surveillance schedule is 
    excessive and does not contribute to improved diesel-generator 
    reliability. Within eight (8) hours, the determination that no 
    common cause failure exists is required to be completed or the 
    operable diesel-generator will be tested. Eight (8) hours is 
    consistent with the guidance provided in NUREG-1366, ``Improvements 
    to Technical Specifications Surveillance Requirements.''
        Technical Specification 4.6.3.e requires that the operable 
    diesel-generator be operated at rated load (i.e., connected to 
    offsite power) to demonstrate its operability in the event any 
    diesel-generator becomes inoperable. As indicated in Information 
    Notice 84-69, when a diesel-generator is operated connected to 
    offsite or non-vital loads, the emergency power system is not 
    independent of disturbances on the non-vital and offsite power 
    systems. Therefore, diesel-generator availability is potentially 
    lessened by a demonstration of operability requiring connection of 
    the diesel-generator to offsite power sources. At a time when at 
    least one diesel-generator is already inoperable, this Surveillance 
    Requirement could add further risk to losing the remaining operable 
    diesel-generator. Therefore, Niagara Mohawk proposes that 
    Surveillance Requirement 4.6.3.e be changed such that a diesel-
    generator does not have to be operated at rated load. These changes 
    will preclude offsite power source disturbances from affecting 
    diesel-generator reliability.
        Existing Technical Specification 4.6.3.e requires that the 
    operable diesel-generator be started immediately in the event a 
    diesel-generator becomes inoperable. The requirement to immediately 
    test a diesel-generator is overly burdensome when compared to more 
    recent diesel-generator Technical Specification requirements. As 
    previously discussed, Niagara Mohawk proposes to add wording to 
    Technical Specification 4.6.3.e to give an operator eight (8) hours 
    to determine whether a common cause failure exists or to test the 
    operable diesel-generator when a diesel-generator is declared 
    inoperable for a reason other than an inoperable support system or 
    preplanned maintenance or testing. Eight (8) hours is consistent 
    with the guidance provided in NUREG-1366, ``Improvements to 
    Technical Specifications Surveillance Requirements.''
        Existing Technical Specification 4.6.3.e requires that the 
    operable diesel-generator be tested immediately and once per week 
    thereafter. Technical Specification 3.6.3.c requires that an 
    inoperable diesel-generator be returned to an operable condition 
    within seven (7) days to meet the Limiting Condition for Operation. 
    Therefore, the requirement to test the operable diesel-generator 
    ``once a week thereafter'' is not applicable. In addition, testing 
    the operable diesel-generator one time is adequate to confirm 
    operability of a diesel-generator. Repetitive testing following 
    initial confirmation of operability is unwarranted. Therefore, 
    Niagara Mohawk proposes to delete the requirement to test the 
    operable diesel-generator weekly following the initial test.
        Because the proposed change does not affect the design or 
    performance of the diesel-generators nor adversely affect the 
    reliability of the diesel-generators, the change will not result in 
    an increase in the consequences of an accident previously evaluated 
    (i.e., Station Blackout analyses). Because this change does not 
    affect the probability of accident precursors, the proposed change 
    does not affect the probability of an accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated
        The proposed change to Technical Specification 4.6.3.e does not 
    introduce any new operating configurations or new accident 
    precursors and does not involve any physical alterations to plant 
    configurations which could initiate a new or different kind of 
    accident. The proposed change does not affect the design or 
    performance characteristics of the diesel-generators nor does the 
    change create the possibility of the loss of both diesel-generators 
    because common cause failure assessments will be performed. The 
    change will delete excessive diesel-generator testing and therefore 
    increase overall plant safety by increasing diesel-generator 
    reliability. Therefore, the proposed amendment will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety
        The proposed change to Technical Specification 4.6.3.e will not 
    reduce the number of emergency power sources required by Technical 
    Specification Limiting Condition for Operation 3.6.3 or affect the 
    normal surveillance requirements as described in Technical 
    Specification 4.6.3. The normal surveillance tests demonstrate 
    acceptable reliability and assure that the operable diesel-generator 
    is capable of performing its intended function. The proposed change 
    to delete the excessive testing requirements does not affect the 
    design or performance of any diesel-generator and does not adversely 
    affect diesel-generator reliability. Eliminating unnecessary testing 
    will potentially increase diesel-generator reliability by reducing 
    the stresses caused by such testing. Therefore, the proposed change 
    does not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Robert A. Capra
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: November 30, 1993
        Description of amendment request: The proposed amendment would 
    change sections 3.2/4.2, Protective Instrumentation, and 3.17/4.17, 
    Control Room Habitability, by deleting the requirements for a chlorine 
    detection system and revises the limiting conditions for operation for 
    the Control Room Ventilation System to be more consistent with Standard 
    Technical Specifications. Due to design changes at the Monticello 
    Nuclear Generating Plant, chlorine is no longer stored onsite as a 
    liquified gas and regulations requiring early warning of an onsite 
    chlorine release do not apply.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Concerning Deletion of Requirements for the Chlorine 
    Detection System
        The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Postulated chemical releases of chlorine have been shown to be 
    such that incapacitation of the control room operators would not 
    occur within allowed time frames for the donning of protective 
    breathing equipment, or that the probability of a chlorine trucking 
    transportation accident which causes incapacitation of control room 
    operators with potential consequences of a radioactive release in 
    excess of 10 CFR 100 guidelines is well below the level of concern 
    as established in regulatory guidance. Therefore, this amendment 
    will not cause a significant increase in the probability or 
    consequences of an accident previously evaluated for the Monticello 
    plant.
        The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The performance of a new toxic chemical analysis for the 
    Monticello site has demonstrated that human detection may be relied 
    upon to detect chlorine toxic chemical releases. Operator protection 
    is established via the donning of protective breathing equipment. 
    The capability to manually isolate the control room with dampers is 
    retained. The ability of the operators to cope with a chlorine toxic 
    gas hazard remains consistent with the protection measures available 
    for other toxic chemicals stored onsite, stored in the vicinity of 
    the site, or transported near the plant site. The proposed amendment 
    will not create the possibility of a new or different kind of 
    accident.
        The proposed amendment will not involve a significant reduction 
    in the margin of safety.
        The performance of a new toxic chemical analysis for the 
    Monticello site has demonstrated that incapacitation of the control 
    room operators would not occur within allowed time frames for the 
    donning of protective breathing equipment and that a postulated 
    hazardous chemical release due to a trucking transportation accident 
    involving chlorine is of a sufficiently low probability of 
    occurrence that it need not be considered. The basis of the chlorine 
    detectors and associated Technical Specifications is to provide 
    protection against an accident scenario which has been demonstrated 
    to be of extremely low probability (a trucking transportation 
    accident involving chlorine within five miles of the plant), 
    therefore removal of the chlorine detectors from the plant design 
    and the associated Technical Specifications will not involve a 
    significant reduction in the margin of safety.
        2. Concerning the Limiting Conditions for Operation for the 
    Control Room Ventilation System and Technical Specification Bases
    
        The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Control Room Ventilation system ensures that Main Control 
    Room habitability is maintained such that personnel and equipment 
    located in the control room can respond to mitigate the consequences 
    of an accident. The system does not contribute to the probability of 
    occurrence of any design basis accident. The operability 
    requirements as proposed for the revised specification 3.17.A ensure 
    that the Control Room Ventilation system is operable during plant 
    conditions for which significant radioactive releases are postulated 
    consistent with the Standard Technical Specification. The proposed 
    changes ensure the Control Room Ventilation system is restored to an 
    operable status or that actions are taken to minimize the importance 
    of the system function within time frames which take into 
    consideration the low probability of an event occurring which would 
    require Control Room Ventilation system function. Therefore, this 
    amendment will not cause a significant increase in the probability 
    or consequences of an accident previously evaluated for the 
    Monticello plant.
        The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The proposed changes to Technical Specifications 3.17.A do not 
    alter the function of the Control Room Ventilation system or its 
    interrelationships with other systems. The proposed changes provide 
    requirements to ensure the Control Room Ventilation system is 
    capable of performing its required function or that actions are 
    taken to minimize the potential for its function being required 
    consistent with regulatory guidance; therefore, this amendment will 
    not create the possibility of a new or different kind of accident 
    from any accident previously analyzed.
        The proposed amendment will not involve a significant reduction 
    in the margin of safety.
        The operability requirements as proposed for the revised 
    specification 3.17.A ensure that the Control Room Ventilation system 
    is operable during plant conditions for which significant 
    radioactive releases are postulated. The performance of a new toxic 
    chemical analysis for the Monticello site has demonstrated that a 
    postulated hazardous chemical release due to a trucking 
    transportation accident involving chlorine is of a sufficiently low 
    probability of occurrence that it need not be considered. As the 
    basis of the chlorine detectors and current operability requirements 
    for the control Room Ventilation system is to provide protection 
    against an accident scenario which has been demonstrated to be of 
    extremely low probability, the proposed revision to the Control Room 
    Ventilation operability requirements will not involve a significant 
    reduction in the margin of safety.
        The proposed changes to Technical Specification 3.17.A ensure 
    that both trains of the Control Room Ventilation system are restored 
    to an operable status within a time frame which takes into 
    consideration the low probability of an event occurring requiring 
    Control Room Ventilation system function, the availability of the 
    redundant Control Room Ventilation train and the capability of the 
    safety related Emergency Filtration Train to pressurize the control 
    room without the Control Room Ventilation system. The proposed 
    changes provide requirements to ensure the Control Room Ventilation 
    system is capable of performing its required function or that 
    actions are taken to minimize the potential for its function to be 
    required consistent with regulatory guidance; therefore, the 
    proposed change will not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: L. B. Marsh
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: January 3, 1994
        Description of amendment request: The proposed amendment would 
    revise the requirements of Technical Specification 4.6.E.1.a, which 
    currently specifies that a minimum of seven safety/relief valves shall 
    be bench checked or replaced with a bench checked valve each refueling 
    outage. The proposed amendment would change this specification to 
    require the valves to be tested in accordance with the Section XI 
    Inservice Testing Requirements of the ASME Boiler and Pressure Vessel 
    Code. The proposed change is consistent with the Improved Standard 
    Technical Specifications, NUREG-1433.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment is limited to changes to the surveillance 
    testing requirements (bench checking or replacement) applicable to 
    the main steam system safety/relief valves. This surveillance 
    requirement is performed while the plant is in a cold shutdown 
    condition at a time when the safety/relief valves are not required 
    to be operable. The performance of this evolution is not an input or 
    consideration in any accident previously evaluated, thus the 
    proposed change will not increase the probability of any such 
    accident occurring. Current safety analyses conclude that the 
    pressure relief capabilities of the Safety Relief valves are 
    adequate assuming that one of the eight safety/relief valves fails 
    to open upon demand. The proposed change will not adversely affect 
    the reliability of the valves and will therefore not reduce the 
    conservatism of this assumption.
        Similarly, the proposed amendment specifies testing requirements 
    consistent with accepted industry codes and regulatory guidance to 
    provide assurance that the valves will function as designed. The 
    amendment will not diminish the capability of the safety/relief 
    valves to perform as required during any accident previously 
    evaluated and will therefore not increase the consequences of any 
    such accident.
        b. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The proposed amendment does not involve any modification to 
    plant equipment or operating procedures, nor will it introduce any 
    new safety/relief valve failure modes that have not been previously 
    considered. The net result of the proposed amendment will be to 
    allow the plant staff the option of decreasing the frequency of 
    safety/relief valve testing to a level that has been acknowledged as 
    acceptable by the ASME Code and NUREG-1433. We therefore conclude 
    the proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously analyzed.
        c. The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The proposed amendment does not involve a decrease in the number 
    or capacity of safety/relief valves that are provided in the system, 
    nor does it involve any change in safety/relief valve setpoints, 
    operability requirements, or limiting conditions for operation. 
    Based on these considerations, we conclude the proposed amendment 
    will not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: L. B. Marsh
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: January 4, 1994
        Description of amendment request: The proposed amendment would 
    change Technical Specifications section 3.11, Reactor Fuel Assemblies, 
    by removing information concerning the analytical method to determine 
    average planar linear heat generation rate (APLHGR) and providing 
    reference to the presentation of the information in the Core Operating 
    Limits Report. In addition, this proposed amendment would change 
    section 6.7, Reporting Requirements, by revising the listing of 
    approved analytical methods for developing the Core Operating Limits 
    Report, and it would revise the Technical Specification Bases for 
    section 3.11 concerning the calculation methodology for MCPR [minimum 
    critical power ratio]. The proposed change to specification 3.11.A 
    would eliminate the duplication of requirements specified in 
    specification 6.7.A.7 and the Core Operating Limits Report for 
    establishing APLHGR limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The APLHGR limits originate from and are associated with LOCA 
    [loss-of-coolant accident] analyses. Standard exposure dependent 
    APLHGR limits are generated from LOCA analyses initiated from rated 
    power and flow conditions. For any allowable off power and off flow 
    condition the APLHGR limit is the smaller of the flow dependent or 
    power dependent limit. These limits are also used in the fuel 
    thermal-mechanical analysis and transient analysis. Flow dependent 
    APLHGR requirements will continue to be established based on 
    analysis and fuel type specific limits determined using NRC approved 
    methodologies to ensure that peak transient average planar heat 
    generation rate during these events is not increased above the fuel 
    design basis values. Power dependent APLHGR limits will continue to 
    be established based on analysis and fuel type specific limits 
    determined using NRC approved methodologies to ensure that peak 
    transient average planar heat generation rate during any transient 
    is not increased above the rated fuel design basis transient values. 
    The proposed amendment establishes appropriate controls to ensure 
    that the APLHGR limits will continue to be determined and 
    established using NRC approved methodology; therefore, this 
    amendment will not cause a significant increase in the probability 
    or consequences of an accident previously evaluated for the 
    Monticello plant.
        The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The proposed amendment does not involve any modifications to 
    plant equipment or operating procedures, nor will it introduce any 
    new failure modes. The proposed amendment ensures that cycle 
    specific APLHGR limits are determined and established using approved 
    methodologies and will not create the possibility of a new or 
    different kind of accident.
        The proposed amendment will not involve a significant reduction 
    in the margin of safety.
        The proposed amendment removes duplication which exists in the 
    Monticello Technical Specification for the identification of the 
    approved analytical methods for establishing the APLHGR core 
    operating limit. In addition the proposed amendment adds the NRC 
    approved Siemens' analytical method for the determination of APLHGR 
    limits based on LOCA/ECCS [emergency core cooling system] analyses. 
    Inclusion of the NRC approved Siemens' analytical method ensures 
    proper coordination of the methodology employed to establish the 
    APLHGR limiting condition for operation for each type of fuel as a 
    function of axial location and average planar exposure. APLHGR 
    limits will continue to be determined using NRC approved methodology 
    as established in specification 6.7.A.7.b. The established APLHGR 
    limits will be verified to be consistent with the accident analysis 
    contained in the Monticello Updated Safety Analysis Report. The 
    proposed amendment will not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: L. B. Marsh
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendments request: September 21, 1992, as revised December 
    29, 1992, and November 24, 1993
        Description of amendments requests: The proposed amendments would 
    change various Technical Specification (TS) sections and associated 
    Bases for surveillance test intervals and allowed outage times for the 
    engineered safety features and reactor protection system 
    instrumentation consistent with the NRC Staff position as documented in 
    NRC letters to the Westinghouse Owners Group.
        The proposed license amendment request also updates operation modes 
    to be consistent with Westinghouse Standard Technical Specification 
    operational modes and also includes several editorial changes to the 
    Prairie Island TS that are unrelated to the changes described above.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The determination that the results of the proposed change are 
    within all acceptable criteria have been established in the SERs 
    prepared for WCAP-10271, WCAP-10271 Supplement 1, WCAP-10271 
    Supplement 2 and WCAP-10271 Supplement 2, Revision 1 issued by 
    References 1, 2, and 5 [of the November 24, 1993, application]. 
    Implementation of the proposed changes is expected to result in an 
    acceptable increase in total Reactor Protection and Engineered 
    Safety Features Systems yearly unavailability. This increase, which 
    is primarily due to less frequent surveillance, results in a[n] 
    increase of similar magnitude in the probability of an Anticipated 
    Transient Without Scram (ATWS) and in the probability of core melt 
    resulting from an ATWS and also results in a small increase in core 
    damage frequency (CD) due to Engineered Safety Features 
    unavailability.
        Implementation of the proposed changes is expected to result in 
    a significant reduction in the probability of core melt from 
    inadvertent reactor trips. This is a result of a reduction in the 
    number of inadvertent reactor trips (0.5 fewer inadvertent reactor 
    trips per unit per year) occurring during testing of Reactor 
    Protection System instrumentation. This reduction is primarily 
    attributable to less frequent surveillance.
        The reduction in inadvertent core melt frequency is sufficiently 
    large to counter the increase in ATWS core melt probability 
    resulting in an overall reduction in total core melt probability.
        The values determined by the Westinghouse Owners Group and 
    presented in the WCAP for the increase in core damage frequency were 
    verified by Brookhaven National Laboratory (BNL) as part of an audit 
    and sensitivity analyses for the NRC Staff. Based on the small value 
    of the increase compared to the range of uncertainty in the core 
    damage frequency, the increase is considered acceptable.
        The changes of an editorial nature, including the change to 
    Standard Technical Specification format for the instrumentation 
    Technical Specifications and mode definitions, have no impact on the 
    severity or consequences of an accident previously evaluated.
        The proposed changes do not result in an increase in the 
    severity or consequences of an accident previously evaluated. 
    Implementation of the proposed changes affects the probability of 
    failure of the Reactor Protection System and Engineered Safety 
    Features but does not alter the manner in which protection is 
    afforded nor the manner in which limiting criteria are established.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The proposed changes do not involve hardware changes and do not 
    result in a change in the manner in which the Reactor Protection 
    System and Engineered Safety Features provide plant protection. No 
    change is being made which alters the functioning of the Reactor 
    Protection System or Engineered Safety Features. Rather the 
    likelihood or probability of the Reactor Protection System or 
    Engineered Safety Features functioning properly is affected as 
    described above. Therefore the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The changes of an editorial nature, including the change to 
    Standard Technical Specification format for the instrumentation 
    Technical Specifications and mode definitions does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        . The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The proposed changes do not alter the manner in which safety 
    limits, limiting safety system setpoints or limiting conditions for 
    operation are determined. The impact of reduced testing other than 
    as addressed above is to allow a longer time interval over which 
    instrument uncertainties (e.g., drift) may act. Experience has shown 
    that the initial uncertainty assumptions are valid for reduced 
    testing.
        Implementation of the proposed changes is expected to result in 
    an overall improvement in safety by:
        a. Less frequent testing will result in less inadvertent reactor 
    trips and actuation of Engineered Safety Features components.
        b. Higher quality repairs leading to improved equipment 
    reliability due to longer repair times.
        c. Improvements in the effectiveness of the operating staff in 
    monitoring and controlling plant operation. This is due to less 
    frequent distraction of the operator and shift supervisor to attend 
    to instrumentation testing.
        The changes of an editorial nature, including the change to 
    Standard Technical Specification format for the instrumentation 
    Technical Specifications and mode definitions [do] not lead to a 
    reduction in any margin of safety.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: L. B. Marsh
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station,Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: December 28, 1993
        Description of amendment request: The proposed amendment to the 
    Technical Specifications would revise the surveillance test frequency 
    from monthly to quarterly for several channel functional tests for 
    Reactor Protective System and Engineered Safety Feature Instrumentation 
    and Controls based on Generic Letter 93-05.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change does not involve significant hazards 
    considerations because operation of Fort Calhoun Station Unit (FCS) 
    No. 1 in accordance with this change would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Increasing the surveillance test interval (STI) from monthly to 
    quarterly for the Reactor Protective System (RPS) and Engineered 
    Safety Features Actuation System (ESFAS) instrumentation has two 
    principal effects with opposing impacts on core melt risk. The first 
    impact is a slight increase in core melt frequency that results from 
    the increased unavailability of the instrumentation in question. The 
    unavailability of the tested instrumentation components is 
    translated to result in a failure of the reactor to trip, an 
    Anticipated Transient Without Scram (ATWS), or a failure of the 
    appropriate engineered safety features to actuate when required. The 
    opposing impact on core melt risk is the corresponding reduction in 
    core melt frequency that would result due to the reduced exposure of 
    the plant to test-induced transients. This results in a net decrease 
    in core melt frequency of approximately 4.1x10-8 per year.
        Representative fault tree models were developed for FCS and the 
    corresponding changes in core melt frequency were quantified in 
    evaluations CEN-327-A and CEN-327-A, Supplement 1. The NRC issued a 
    Safety Evaluation Report (SER) which found that these evaluations 
    were acceptable for justifying the extensions in the STIs for the 
    RPS and ESFAS from 30 days to 90 days and that the RPS 
    unavailabilities resulting from extending the STIs were not 
    considered to be significant. Estimates of the reduction in scram 
    frequency from the reduction in test-induced scrams and the 
    corresponding reduction in core melt frequency were found 
    acceptable. STIs of 90 days were found to result in a net reduction 
    in core melt risk.
        A plant specific calculation/setpoint drift analysis was 
    conducted, as required by the NRC SER, that analyzed the effect on 
    instrument drift of extending the RPS and ESF instrumentation and 
    controls functional STI from monthly to quarterly. The results 
    demonstrated that the observed changes in instrument uncertainties 
    for the extended STI do not exceed the current 30-day setpoint 
    assumptions. Therefore, it is unnecessary to change any setpoints to 
    accommodate the proposed extended STI.
        Operation of the facility in accordance with this proposed 
    change, therefore, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed change does not involve any changes in equipment 
    and will not alter the manner in which the plant will be operated. 
    RPS and ESFAS setpoints will not be changed as the instrument 
    uncertainties resulting from the proposed STI (calculated using 
    actual plant data) are less than the instrument uncertainties 
    assumed for 30 days. Thus, this proposed change will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        (3) Involve a significant reduction in a margin of safety.
        There are no changes to the equipment or plant operations. RPS 
    and ESFAS setpoints will not be changed as the instrument 
    uncertainties resulting from the proposed STI (calculated using 
    actual plant data) are less that the instrument uncertainties 
    assumed for 30 days.
        Implementation of the proposed changes is expected to result in 
    an overall improvement in plant safety due to the fact that reduced 
    testing intervals will result in fewer inadvertent reactor trips and 
    less frequent actuation of ESFAS components. The conclusions of the 
    accident analyses in the FCS Updated Safety Analysis Report (USAR) 
    remain valid and the safety limits continue to be met. Thus, this 
    proposed change does not reduce a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: LeBoeuf, Lamb, Leiby, and MacRae, 1875 
    Connecticut Avenue, N.W., Washington, D.C. 20009-5728NRC Project 
    Director:
        William D. Beckner
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: December 28, 1993
        Description of amendment request: The proposed amendment to the 
    James A. FitzPatrick Technical Specifications (TSs) clarifies Limiting 
    Condition for Operation (LCO) 3.5.D.4. Amendment No. 179 to the TS 
    added LCO 3.5.D.4 to permit hydrostatic and leakage testing at 
    temperatures up to 300 deg.F without requiring certain equipment, 
    including the automatic depressurization system (ADS), to be operable. 
    However, LCO 3.5.D.4 can be mistakenly interpreted to require the ADS 
    be operable at temperatures less than 212 deg.F. Requiring the ADS to 
    be operable during hydrostatic and leakage testing with temperatures 
    below 212 deg.F was clearly not the intent of Amendment No. 179. The 
    proposed change will clarify LCO 3.5.D.4 to resolve this concern.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The plant accident analyses are not affected by the proposed 
    Technical Specification change. Prior to implementation of Amendment 
    179, hydrostatic and leakage testing of the RCS was performed with 
    reactor coolant temperatures below 212 deg.F while the ADS was 
    inoperable. Amendment 179 revised the Technical Specifications in 
    anticipation of increased pressure temperature limits requiring 
    hydrostatic and leakage testing at or above 212 deg.F. Requiring the 
    ADS to be operable during hydrostatic or leakage testing with 
    temperatures below 212 deg.F was clearly not the intent of Amendment 
    179. The change will not increase the probability or consequences of 
    previously evaluated accidents.
        2. create the possibility of a new or different kind of accident 
    from those previously evaluated.
        The proposed change involves no modifications to hardware, 
    analyses, operations or procedures. The change clarifies LCO 3.5.D.4 
    to allow hydrostatic and leakage testing of the RCS below 300 deg.F 
    without requiring the ADS to be operable. The change is 
    administrative in nature since it only clarifies the intent of the 
    Technical Specifications as agreed to with the NRC and cannot create 
    a new or different kind of accident.
        3. involve a significant reduction in the margin of safety.
        The proposed change will not affect any plant safety margins. 
    The existing plant accident analyses are not affected by the 
    proposed change. This revision of LCO 3.5.D.4 is intended to clarify 
    that the ADS is not required to be operable during hydrostatic or 
    leakage testing of the RCS. This position is substantiated by the 
    NRC safety evaluation for Amendment 179 which acknowledges that 
    hydrostatic and leakage testing can not be performed without making 
    the ADS, and other systems, inoperable.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Robert A. Capra
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: January 31, 1994
        Description of amendment request: The proposed amendment to the 
    James A. FitzPatrick Technical Specifications would revise the limiting 
    conditions for operation (LCO), surveillance requirements, and Bases 
    section for the main condenser steam jet air ejectors (SJAE). The 
    proposed changes correct a typographical error, clarify the modes of 
    operation during which the SJAE LCOs and surveillance requirements are 
    applicable, revise the action required upon entering a SJAE LCO, and 
    establish a threshold level below which there will be no requirement to 
    perform grab samples and isotopic analyses of SJAE effluent.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed amendment revision involves no hardware changes, no 
    changes to the operation of any systems or components and no changes 
    to structures. The changes clarify the Technical Specifications by 
    specifying the modes of operation during which the LCOs and 
    Surveillance Requirements of Specification 3.5 are applicable. The 
    changes also include specific guidance for the operators to prevent 
    or minimize the release of radioactive gases to the environment. 
    These changes can not cause an increase in the probability of, nor 
    alter the consequences of, an accident previously evaluated.
        The establishment of a threshold below which grab samples are 
    not required will alter procedures by allowing SJAE operation 
    without grab samples to determine effluent content at low levels of 
    radioactivity (i.e., less than 5,000 micro Ci/sec). This will not 
    affect the monitoring system's ability to detect, alarm, and isolate 
    the offgas system if the concentration of radioactive material in 
    the effluence reaches the appropriate setpoint.
        The surveillance requirement for taking a grab sample after a 
    greater than 50% increase in release rate is intended to assist 
    operators in determining if there is any increase in fuel failure 
    during steady state operations. This would assure that routine 
    operational limits are maintained. The grab samples do not provide 
    any automatic protective function (e.g., MSIV [main steam isolation 
    valve] or Offgas System isolation) for mitigating an accident but 
    provide radionuclide concentration data.
        The performance of SJAE effluent grab samples is not credited 
    towards detecting nor mitigating any design basis accidents since 
    spontaneous fuel failure is not a FSAR [Final Safety Analysis 
    Report] accident initiator but a consequence of an accident. 
    Therefore, the use of a 5,000 micro Ci/sec threshold, which is 
    approximately 1% of the trip setpoint, would not alter the 
    consequences or probabilities of established accident scenarios.
        2. create the possibility of a new or different kind of accident 
    from those previously evaluated.
        The proposed changes provide improved clarity concerning 
    applicability of the specifications and specific guidance for 
    preventing/mitigating the release of radioactive gases to the 
    environment. The proposed changes also provide guidance for limiting 
    the number of unnecessary grab samples.
        These changes do not affect the manner in which the main 
    condenser steam jet air ejector is operated. The proposed changes to 
    the Technical Specifications reflect either established plant 
    practice (i.e., applicable modes or mitigation procedures) or new 
    surveillance guidelines to minimize unnecessary grab samples. In all 
    cases, the proposed changes have no affect on any parameters which 
    would be considered or used in an accident analysis. The changes, 
    therefore, do not pose a safety issue different from those analyzed 
    previously for the FSAR.
        3. involve a significant reduction in the margin of safety.
        The proposed changes to the Technical Specifications will not 
    alter the intent of the surveillance requirement to monitor for the 
    possibility of fuel failure. Considering the difference between the 
    proposed threshold value and the current alarm setpoint, a reduction 
    in grab samples during plant operation with low concentrations of 
    radioactivity in the primary coolant will not affect any plant 
    safety margins.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Robert A. Capra
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: January 31, 1994
        Description of amendment request: The proposed amendment to the 
    James A. FitzPatrick Technical Specifications would revise 
    Specification 3.8 to adopt the Limiting Conditions for Operation (LCO) 
    of Section 3/4.7.6, ``Sealed Source Contamination,'' as stated in 
    NUREG-0123, ``Standard Technical Specifications for General Electric 
    Boiling Water Reactors (BWR/5)'' (STS). In addition, the proposed 
    change reformats Specifications 3.8 and 4.8 to make them consistent 
    with the remainder of the FitzPatrick Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Adopting the LCO described in the ``Sealed Source 
    Contamination'' section of NUREG-0123 (STS) does not increase the 
    probability or the consequences of an accident or malfunction of a 
    safety-related structure, system, or component previously reviewed 
    in the FSAR [Final Safety Analysis Report]. The proposed changes do 
    not increase the probability of causing, either directly or 
    indirectly an uncontrolled release of significant amounts of 
    radiation. Deleting 10 CFR 30.71 as the basis for exempting sealed 
    sources for the leak testing requirements removes a requirement that 
    is redundant to other federal regulations requirements. The proposed 
    changes to reformat Specifications 3.8 and 4.8 are administrative in 
    nature and do not increase the probability or consequences of an 
    accident previously evaluated in the FSAR. Therefore, the proposed 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes do not alter the radioactive materials 
    controls established at the restricted area boundaries and do not 
    increase the amount of radioactive materials on site. There are no 
    modifications to safety systems as a result of the proposed changes. 
    Therefore, the proposed changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated in the FSAR.
        3. involve a significant reduction in a margin of safety.
        Adopting the wording of the STS regarding the sealed sources 
    limiting conditions for operations will not reduce the ability of 
    the operators to detect a leaking sealed radioactive source. 
    Established radiological controls (i.e., handling techniques and 
    good health physics practices) implemented through plant procedures 
    will ensure that the sealed sources will continue to be tested as 
    required by the Technical Specifications and applicable regulations. 
    The proposed changes do not alter the radioactive materials controls 
    established at the restricted area boundary and do not increase the 
    amount of radioactive materials on site. Therefore, the proposed 
    changes do not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Robert A. Capra
    
    Sacramento Municipal Utility District, Docket No. 50-312, Rancho 
    Seco Nuclear Generating Station, Sacramento County, California
    
        Date of amendment request: December 9, 1993
        Description of amendment request: The proposed amendment would 
    change the Rancho Seco Permanently Defueled Technical Specifications 
    (PDTS) to implement and ensure consistency with the revisions in 10 CFR 
    Part 20.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A significant increase in the probability or 
    consequences of an accident previously evaluated in the SAR (Safety 
    Analysis Report) will not be created, because the proposed changes 
    are editorial in nature, are designed to implement the 10 CFR Part 
    20 regulations, and have no affect on any accidents evaluated in the 
    Rancho Seco Defueled Safety Analysis Report (DSAR), i.e., the 
    dropped fuel assembly accident, the loss of offsite power condition, 
    or a radwaste tank rupture.
        PA-187 (Proposed Amendment) will not create the 
    possibility of a new or different type of accident evaluated in the 
    SAR, because the changes are editorial in nature, implement the new 
    10 CFR Part 20 radiation protection regulations, and do not provide 
    any new mechanisms by which an accident can occur.
        The proposed PDTS amendment will not involve a 
    significant reduction in the margin of safety, because the District 
    will continue to maintain the appropriate radiation protection 
    controls, through implementation of the new 10 CFR Part 20 
    regulations, that are necessary to ensure Rancho Seco continues to 
    be operated safely from a personnel radiation exposure standpoint 
    during the Permanently Defueled Mode.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Central Library, Government 
    Documents 828 I Street, Sacramento, California 95814.
        Attorney for licensee: Dana Appling, Esquire, Sacramento Municipal 
    Utility District, P.O. Box 15830, Sacramento, California 95852-1830
        NRC Project Director: Seymour H. Weiss
    
    Tennessee Valley Authority, Docket No. 50-328, Sequoyah Nuclear 
    Plant, Unit 2, Hamilton County, Tennessee
    
        Date of amendment request: February 8, 1994 (TS 94-02)
        Description of amendment request: The proposed change would revise 
    Operating License Condition 2.C.(17) to temporarily extend the 
    surveillance interval for certain specified instruments from the normal 
    18-month interval to a maximum of 28 months for 18-month surveillances 
    and 46 months for the 3-year Containment fire hose hydrostatic 
    surveillance test in order to prevent exceeding the allowable testing 
    frequency prior to the refueling outage that has been rescheduled to 
    start in July 1994.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change is temporary and allows a one-time extension 
    of specific surveillance requirements (SRs) for Cycle 6 to allow 
    surveillance testing to coincide with the sixth refueling outage. 
    The proposed surveillance interval extension is short and will not 
    cause a significant reduction in system reliability nor affect the 
    ability of the systems to perform their design function. Current 
    monitoring of plant conditions and continuation of the surveillance 
    testing required during normal plant operation will continue to be 
    performed to ensure conformance with TS operability requirements. 
    Therefore, this change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        Extending the surveillance interval for the performance of 
    specific testing will not create the possibility of any new or 
    different kind of accidents. No changes are required to any system 
    configurations, plant equipment, or analyses. Therefore, this change 
    will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        Surveillance interval extensions will not impact any plant 
    safety analyses since the assumptions used will remain unchanged. 
    The safety limits assumed in the accident analyses and the design 
    function of the equipment required to mitigate the consequences of 
    any postulated accidents will not be changed since only the 
    surveillance test interval is being extended. Historical performance 
    generally indicates a high degree of reliability, and surveillance 
    testing performed during normal plant operation will continue to be 
    performed to verify proper performance. Therefore, the plant will be 
    maintained within the analyzed limits, and the proposed extension 
    will not significantly reduce the margin of safety.
        The NRC has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: December 23, 1992
        Description of amendment request: The proposed amendment would 
    revise TS 3/4 3.3.5 and its Bases adding testing requirements for 
    transfer switches used to meet 10 CFR Part 50, Appendix R (Fire 
    Protection) requirements and specifies a new special report requirement 
    for TS 6.9.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below, indicating that the proposed 
    changes would:
        1a. Not involve a significant increase in the probability of an 
    accident previously evaluated because none of the proposed changes 
    are associated with the initiation of any design bases accident. The 
    addition of Limiting Condition for Operation (LCO) 3.3.3.5.2 and 
    Surveillance Requirement (SR) 4.3.3.5.2 to the Technical 
    Specifications will require each control circuit and transfer switch 
    that is required for a serious control room or cable spreading room 
    fire to be operable during Modes 1, 2 and 3 and to be verified at 
    least once per 18 months as capable of performing the intended 
    function. New Action b will require restoration of an inoperable 
    control circuit or transfer switch (required for a serious control 
    room or cable spreading room fire) within 30 days or a Special 
    Report submitted to the NRC pursuant to Specification 6.9.2 within 
    the next 30 days. Surveillance testing procedures will be prepared, 
    reviewed and approved in accordance with Technical Specification 
    (TS) 6.5.3, Technical Review and Control, which will ensure an 
    unreviewed safety question is not created. To support the addition 
    of the new LCO, Action and SR, the existing LCO, Action and SR are 
    proposed to be administratively re-numbered or re-lettered. The new 
    Special Report requirement is proposed to be administratively added 
    to TS 6.9.2.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because no equipment, accident 
    conditions, or assumptions are affected which could lead to 
    significant increases in radiological consequences. The addition of 
    LCO 3.3.3.5.2 and SR 4.3.3.5.2 to the Technical Specifications will 
    require each control circuit and transfer switch that is required 
    for a serious control room or cable spreading room fire to be 
    operable during Modes 1, 2 and 3 and to be verified at least once 
    per 18 months as capable of performing the intended function. New 
    Action b will require restoration of an inoperable control circuit 
    or transfer switch (required for a serious control room or cable 
    spreading room fire) within 30 days or a Special Report submitted to 
    the NRC pursuant to Specification 6.9.2 within the next 30 days. 
    Surveillance testing procedures will be prepared, reviewed and 
    approved in accordance with Technical Specification (TS) 6.5.3, 
    which will ensure an unreviewed safety question is not created. To 
    support the addition of a new LCO, Action and SR, the existing LCO, 
    Action and SR are proposed to be administratively re-numbered or re-
    lettered. The new Special Report requirement is proposed to be 
    administratively added to TS 6.9.2.
        2a. Not create the possibility of a new kind of accident from 
    any accident previously evaluated because no new accident initiators 
    are introduced by the proposed changes. The addition of LCO 
    3.3.3.5.2 and SR 4.3.3.5.2 to the Technical Specifications will 
    require each control circuit and transfer switch that is required 
    for a serious control room or cable spreading room fire to be 
    operable during Modes 1, 2 and 3 and to be verified at least once 
    per 18 months as capable of performing the intended function. New 
    Action b will require restoration of an inoperable control circuit 
    or transfer switch (required for a serious control room or cable 
    spreading room fire) within 30 days or a Special Report submitted to 
    the NRC pursuant to Specification 6.9.2 within the next 30 days. 
    Surveillance testing procedures will be prepared, reviewed and 
    approved in accordance with TS 6.5.3, which will ensure an 
    unreviewed safety question is not created. To support the addition 
    of the new LCO, Action and SR, the existing LCO, Action and SR are 
    proposed to be administratively re-numbered or re-lettered. The new 
    Special Report requirement is proposed to be administratively added 
    to TS 6.9.2.
        2b. Not create the possibility of a different kind of accident 
    from any accident previously evaluated because no different accident 
    initiators are introduced by the proposed changes. The addition of 
    LCO 3.3.3.5.2 and SR 4.3.3.5.2 to the Technical Specifications will 
    require each control circuit and transfer switch that is required 
    for a serious control room or cable spreading room fire to be 
    operable during Modes 1, 2, and 3 and to be verified at least once 
    per 18 months as capable of performing the intended function. New 
    Action b will require restoration of an inoperable control circuit 
    or transfer switch (required for a serious control room or cable 
    spreading room fire) within 30 days or a Special Report submitted to 
    the NRC pursuant to Specification 6.9.2 within the next 30 days. 
    Surveillance testing procedures will be prepared, reviewed and 
    approved in accordance with TS 6.5.3, which will ensure an 
    unreviewed safety question is not created. To support the addition 
    of the new LCO, Action and SR, the existing LCO, Action and SR are 
    proposed to be administratively re-numbered or re-lettered. The new 
    Special Report requirement is proposed to be administratively added 
    to TS 6.9.2.
        3. Not involve a significant reduction in a margin of safety 
    because these are not new or significant changes to the initial 
    conditions contributing to accident severity or consequences, 
    therefore, there are no significant reductions in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, N.W., Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: September 24, 1993
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications to extend the reporting period of the 
    Semiannual Radioactive Effluent Release Report from semiannually to 
    annually. Additionally, the report submission date would change from 60 
    days after January 1 and July 1 of each year to before May 1 of each 
    year. The changes to the reporting period and report date are being 
    made to implement the August 31, 1992, amendment to 10 CFR 50.36a. The 
    affected Technical Specifications Sections are 1.18, 3.11.1.4, 
    3.11.2.6, 6.9.1.7, 6.14c, and the Index.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve a significant hazards 
    consideration because operation of Callaway Plant with these changes 
    would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes do not affect accident initiators or 
    assumptions. The radiological consequences of any accident 
    previously evaluated remain unchanged.
        (2)Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        These changes do not impact any administrative controls nor do 
    they involve physical alterations to the plant with respect to 
    radioactive effluent. There is no new type of accident or 
    malfunction created and the method and manner of plant operation 
    will not change.
        (3) Involve a significant reduction in a margin of safety.
        The margin of safety remains unaffected since no design change 
    is made and plant operation remains the same. The proposed changes 
    do not affect any safety limits or boundary or system performance.
        As discussed above, the proposed changes are strictly 
    administrative in nature and have no affect on plant operations. 
    They do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated or create the 
    possibility of a new or different kind of accident from any 
    previously evaluated. These changes do not result in a significant 
    reduction in a margin of safety. Therefore, it has been determined 
    that the proposed changes do not involve a significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: John N. Hannon
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: October 6, 1993
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications Section 3.8.3, Electrical Power Systems 
    - Onsite Power Distribution, to make the limiting conditions for 
    operation for four emergency busses (NG05E, NG06E, NG07, and NG08) 
    consistent with other technical specifications. The proposed revision 
    would make the allowed outage time (AOT) for any of these emergency 
    busses 72 hours. This is equivalent to the AOT for one train of the ESW 
    per Technical Specification 3.7.4 and equivalent to the AOT for one 
    train of the UHS cooling tower per Technical Specification 3.7.5.
        This amendment request also proposes an editorial change by 
    removing the number sign () before each electrical bus, 
    battery, and battery charger listed in Technical Specifications Section 
    3.8.3 in order to clarify the specifications and make the nomenclature 
    consistent with other sections.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve a significant hazards 
    consideration because operation of the Callaway Plant with these 
    changes would not:
        (1)Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The implementation of the proposed technical specification 
    changes does not involve any modifications to the physical plant. 
    Even though the MCCs themselves will have an allowed outage time of 
    72 hours instead of 8 hours, the operability requirements of the ESW 
    system itself have not been lessened. The addition of LCs NG07 and 
    NG08 to the technical specifications and surveillances serves to 
    clarify the 480-volt power supply requirements in the technical 
    specifications. The proposed changes do not affect accident 
    initiators or assumptions. The radiological consequences of any 
    accident previously evaluated remain unchanged.
        (2)Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        As noted above, the proposed change eliminates inconsistent 
    requirements from the technical specifications, but overall does not 
    lessen the requirements on ESW system operability imposed by the 
    technical specifications. The implementation of the proposed 
    technical specification changes do not involve any modifications to 
    the physical plant or any significant change to the methods of 
    operation of plant systems. The proposed changes do not create any 
    new accident initiators.
        (3)Involve a significant reduction in a margin of safety.
        The requirements of Technical Specification 3.7.4, Plant Systems 
    - Essential Service Water System, provide specific limiting 
    conditions for operation applicable to the ESW System. In accordance 
    with the definition of operability contained in the technical 
    specifications, the operability of the ESW MCCs has always been 
    included within these requirements. The existing technical 
    specification requirements for onsite A.C. power distribution 
    systems are intended to assure the availability of A.C. power 
    sources supplying multiple safety systems. The NG05E and NG06E MCCs 
    identified by this proposed change provide power for a single safety 
    system (ESW) and associated equipment. The use of the 72 hour limit 
    for the ESW MCCs is consistent with the requirements of Regulatory 
    Guide 1.93, ``Availability of Electrical Power Sources'' and has an 
    insignificant impact on the Callaway Probabilistic Risk Analysis. 
    LCs NG07 and NG08 also only provide power for a single safety system 
    (ESW) and associated equipment (UHS cooling tower). Since the 
    technical specification requirements relative to the ESW system 
    operability are not lessened by this change, there will be no 
    reduction in the margin of safety as defined in the basis for the 
    technical specifications.
        As discussed, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated or create the possibility of a new or different 
    kind of accident from any previously evaluated. These changes do not 
    result in a significant reduction in a margin of safety. Therefore, 
    it has been determined that the proposed changes do not involve a 
    significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: John N. Hannon
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: February 1, 1994
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specifications 
    (TS) by removing the review of the Emergency Plan and its implementing 
    procedures from the list of responsibilities of the Plant Operations 
    Review Committee (PORC). Guidance for this change was provided in 
    Generic Letter 93-07, ``Modification of the Technical Specification 
    Administrative Control Requirements for Emergency and Security Plans,'' 
    dated December 28, 1993. Several other administrative TS changes are 
    proposed including removing specific titles from the list of PORC 
    members in TS 6.5.a.2 and deleting TS 6.5.b which describes the 
    Corporate Support Staff.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        The proposed changes were revised in accordance with the 
    provision of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The likelihood that an accident will occur is neither increased 
    or decreased by these TS changes. These TS changes will not impact 
    the function or method of operation of plant equipment. Thus, there 
    is not a significant increase in the probability of a previously 
    analyzed accident due to these changes. No systems, equipment, or 
    components are affected by the proposed changes. Thus, the 
    consequences of the malfunction of equipment important to safety 
    previously evaluated in the Updated Safety Analysis Report (USAR) 
    are not increased by these changes.
        The proposed changes are administrative in nature and, 
    therefore, have no impact on accident initiators or plant equipment, 
    and thus, do not affect the probabilities or consequences of an 
    accident.
        2)create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        Operation of the facility in accordance with the proposed TS 
    changes would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed changes do not involve changes to the physical 
    plant or operations. Since these administrative changes do not 
    contribute to accident initiation, they do not produce a new 
    accident scenario or produce a new type of equipment malfunction. 
    Also, these changes do not alter any existing accident scenarios; 
    they do not affect equipment or its operation, and thus, do not 
    create the possibility of a new or different kind of accident.
        3)involve a significant reduction in the margin of safety.
        Operation of the facility in accordance with the proposed TS 
    would not involve a significant reduction in a margin of safety. The 
    proposed changes do not affect the plant equipment or operation. The 
    requirements previously contained in the TS's that are being deleted 
    are redundant and are contained in other controlled documents. 
    Safety limits and limiting safety system settings are not affected 
    by these proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: John N. Hannon
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: January 10, 1994, as 
    supplemented February 3, 1994 (Reference LAR 94-01)
        Brief description of amendment request: The proposed amendments 
    would revise the combined Technical Specifications (TS) for the Diablo 
    Canyon Power Plant Unit Nos. 1 and 2 to change TS 3/4.3.2, ``Engineered 
    Safety Features Actuation System Instrumentation,'' and TS 3/4.6.2.3, 
    ``Containment Cooling System.'' TS 3/4.3.2 would be revised to expand 
    the mode applicability to include Mode 4 for the high-high containment 
    pressure signal. TS 3/4.6.2.3 would be revised to clarify acceptable 
    containment fan cooling unit (CFCU) configurations that satisfy the 
    safety analysis requirements and to clarify the minimum required 
    component cooling water flow supplied to the CFCU cooling coils.
        Date of individual notice in Federal Register: January 28, 1994 (59 
    FR 4121)
        Expiration date of individual notice: February 28, 1994
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: November 11, 1993
        Brief description of amendments: The amendments revise the 
    Technical Specifications (TSs) for both Units 1 and 2 by relocating the 
    tables of response time limits for the Reactor Protection System and 
    the Engineered Safety Features Actuation System instruments from the 
    TSs to the Updated Final Safety Analysis Report. These amendments are a 
    ``line-item'' TSs improvement and follow the guidance of Generic Letter 
    93-08, ``Relocation of Technical Specification Tables of Instrument 
    Response Time Limits.''
        Date of issuance: February 10, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
    
        Amendment Nos.:  184 and 161
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67841) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated February 10, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Dates of application for amendments: December 31, 1992, as 
    supplemented June 10, 1993, and August 23, 1993, and December 8, 1993.
        Brief description of amendments: The amendments change the 
    Technical Specifications to (1) revise the definition of core 
    alteration in section 1.0, Definitions, (2) clarify the TS 3/4.9.3, 
    Control Rod Position, in the action statement, surveillance 
    requirements and associated bases, and (3) revise the frequency for the 
    channel calibration of the High Pressure Core Injection Steam Line 
    Tunnel Temperature - High instrument.
        Date of issuance: February 8, 1994
        Effective date: February 8, 1994
    
        Amendment Nos.:  168 and 199
        Facility Operating License Nos. DPR-71 and DPR-62. Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 ( 56 FR 
    36426), and January 5, 1994 (59 FR 617). The June 10, 1993, and August 
    23, 1993, letters provided supplemental information and updated TS 
    pages and did not change the initial proposed no significant hazards 
    consideration determinations. The Commission's related evaluation of 
    the amendments is contained in a Safety Evaluation dated February 8, 
    1994.No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of application for amendments: January 4, 1991, as 
    supplemented on June 24, 1991, December 19, 1991, and October 15, 1993.
        Brief description of amendments: The amendments (a) replace the 
    current fire protection license condition in
        Facility Operating License Nos. DPR-71 and DPR-62 with the standard 
    license conditon in Generic Letter 86-10 and (b) change the Technical 
    Specifications to relocate the fire protection requirements to the 
    BSEP, Units 1 and 2, Updated Final Safety Analysis Report.
        Date of issuance: February 10, 1994
        Effective date: February 10, 1994
    
        Amendment Nos.:  169 and 200
        Facility Operating License Nos. DPR-71 and DPR-62. The amendments 
    replace the current fire protection license condition in
        Facility Operating License Nos. DPR-71 and DPR-62 with the standard 
    license conditon in NRC Generic Letter 86-10, ``Implementation of Fire 
    Protection Requirements.''
        Date of notices in Federal Register: March 20, 1991 (56 FR 11722) 
    and February 5, 1992 (57 FR 4485) The Commission's related evaluation 
    of the amendments is contained in a Safety Evaluation dated February 
    10, 1994.No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: July 26, 1993
        Brief description of amendment: The amendment makes three specific 
    changes in the TS: (1) incorporates the auxiliary feedwater (AFW) flow 
    control valve (FCV) automatic opening feature in periodic surveillance 
    testing, and clarifies in the AFW Bases that given the FCVs auto-open 
    design feature, (2) deletes periodic surveillance testing of the auto-
    closure feature for the AFW motor-driven pump recirculation line 
    valves; and (3) revises the general description of the AFW Bases so 
    they are more concise and address directly the basis of the 
    surveillance requirements.
        Date of issuance: February 14, 1994
        Effective date: February 14, 1994
        Amendment No.: 42
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46225) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 14, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station Units 1 and 2, Lake County, Illinois
    
        Date of application for amendments: November 19, 1993
        Brief description of amendments: The amendment revises the 
    Technical Specifications by changing the reactor vessel low temperature 
    overpressure protection setpoint.
        Date of issuance: February 14, 1994
        Effective date: February 14, 1994
        Amendment Nos.: 153 and 141
        Facility Operating License Nos. DPR-39 and DPR-48. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67842) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 14, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: August 9, 1991, as supplemented 
    by letters dated February 12, 1992, November 8, 1993, and January 25, 
    1994.
        Brief description of amendment: The amendment would revise the 
    Technical Specifications to delete the surveillance requirements and 
    limiting operating conditions for the independent electrical turbine 
    overspeed protection system and to extend the surveillance test 
    interval for the turbine stop and control valves from monthly to an 
    interval of not greater than yearly. Also included is a minor 
    correction to a typographical error.
        Date of issuance: February 8, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 168
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 16, 1991 (56 FR 
    51922) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 8, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: November 4, 1993
        Brief description of amendments: The amendments change the 
    Technical Specifications to allow extended outage time for each train 
    of the control area ventilation system to allow system maintenance to 
    improve system reliability. The one time extension to 14 days (for each 
    train, one at a time) will allow completion of the maintenance 
    activities while one or both units are on-line; otherwise, it would be 
    necessary to shut down both units to complete the maintenance 
    activities or to divide the maintenance activities into less than 7-day 
    segments, which would increase unavailability of the control area 
    ventilation system.
        Date of issuance: February 10, 1994
        Effective date: February 10, 1994
        Amendment Nos.: 140 and 122
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1993 (58 
    FR 62155) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 10, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Duke Power Company, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina 
    Date of application of amendments: November 11, 1993, as 
    supplemented November 22, 1993
    
        Brief description of amendments: The amendments provide an interim 
    acceptance criteria for control rod drop time on Oconee, Unit 1.
        Date of Issuance: February 9, 1994
        Effective date: February 9, 1994
        Amendment Nos.: 205, 205, and 202
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: November 29, 1993 (58 
    FR 62689) The November 22, 1993, letter provided clarifying information 
    that did not change the scope of the November 11, 1993, application and 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 9, 1994. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: June 14, 1990, as supplemented 
    November 17, 1993
        Brief description of amendments: These amendments revise the 
    Electrical Power System Shutdown, the AC Distribution - Shutdown, and 
    the DC Distribution - Shutdown Specifications to more closely resemble 
    the wording contained in the Standard Technical Specifications. The 
    November 17, 1993, supplement changed existing terminology used to 
    designate two emergency busses in Unit No. 1 and two DC busses in Unit 
    2 to standard nomenclature.
        Date of issuance: February 7, 1994
        Effective date: February 7, 1994
        Amendment Nos.:  180 and 60
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 19, 1990 (55 
    FR 38601) The November 17, 1993, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated February 7, 
    1994.No significant hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Florida Power and Light Company, Docket No. 50-335, St. Lucie 
    Plant, Unit No. 1, St. Lucie County, Florida
    
        Date of application for amendment: August 23, 1993
        Brief description of amendment: This amendment will delete the 
    option of using a movable incore detector to determine Incore 
    Instrumentation System operability from the provisions of Technical 
    Specification 3.3.3.2.
    
        Date of issuance: February 8, 1994
        Effective date: February 8, 1994
        Amendment No.: 64
        Facility Operating License No. DPR-67: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 13, 1993 (58 FR 
    52985) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 8, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of applications for amendment: May 26 and December 2, 1993
        Brief description of amendment: The amendment revises the TMI-1 
    Technical Specifications to correct the definition of flood stage. The 
    amendment also revises the TMI-1 Technical Specifications to remove the 
    limiting conditions for operation and surveillance requirements for the 
    Chlorine Detection Systems. Because this bridge was underwater during 
    the 1972 flooding, the reference datum point location will be specified 
    as the Susquehanna River Gage at Harrisburg. TMI-1 removed the gaseous 
    chlorine system for the Circulating Water and River Water Systems.
        Date of issuance: February 10, 1994
        Effective date: As of its date of issuance.
        Amendment No.: 182
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59750) and January 5, 1994 (59 FR 621).The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    February 10, 1994.No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: December 16, 1992, as 
    supplemented December 22, 1993.
        Brief description of amendments: The amendments revise the licenses 
    to allow the replacement of portions of the current Reactor Protection 
    System instrumentation with a digital signal processing system.
        Date of issuance: February 7, 1994
        Effective date: February 7, 1994
        Amendment Nos.: 175 & 160
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments add a 
    license condition to the Operating Licenses.
        Date of initial notice in Federal Register: March 3, 1993 (58 FR 
    12263) The December 22, 1993, letter provided clarifying information 
    which did not change the staff's initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    February 7, 1994. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: August 4, 1993
        Brief description of amendment: The amendment incorporates an 
    additional Emergency Diesel Generator Surveillance Requirement, 
    4.8.1.1.2.C.8, items a, b, and c, to the Technical Specification 
    Section 3/4.8, ``Electrical Power Systems.'' The change requires 
    starting the EDG, with offsite power available, as a result of a Safety 
    Injection Actuation Signal.
        Date of issuance: February 14, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 171
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67852) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 14, 1994. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Thames Valley State Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360.
    
    Pennsylvania Power and Light Company, Docket No. 50-388, 
    Susquehanna Steam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendment: August 19, 1992, as supplemented 
    by letters dated May 18 and October 7, 1993
        Brief description of amendment: The amendment changed the Technical 
    Specifications to revise the logic which controls the automatic 
    transfer of the High Pressure Coolant Injection pump suction source on 
    high suppression pool level.
        Date of issuance: February 9, 1994
        Effective date: February 9, 1994
        Amendment No.: 101
        Facility Operating License No. NPF-22. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 16, 1992 (57 
    FR 42778) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 9, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick 
    Generating Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of application for amendment: August 27, 1993, supplemented by 
    letter dated November 17, 1993
        Brief description of amendment: The amendment allows an expanded 
    operating domain for the Limerick Generating Station (LGS), Unit 1, 
    resulting from the implementation of the Average Power Range Monitor - 
    Rod Block Monitor Technical Specifications/Maximum Extended Load Line 
    Limit Analysis.
        Date of issuance: February 10, 1994
        Effective date: February 10, 1994
        Amendment No. 66
        Facility Operating License No. NPF-39. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 13, 1993 (58 FR 
    52992) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 10, 1994. No 
    significant hazards consideration comments received:
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick 
    Generating Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of application for amendment: November 30, 1993
        Brief description of amendment: This amendment changes the Appendix 
    A technical specifications by allowing the third Type A Containment 
    Integrated Leakage Rate Test in the first 10-year service period to be 
    conducted at Refuel 6.
        Date of issuance: February 16, 1994
        Effective date: February 16, 1994
        Amendment No. 67
        Facility Operating License No. NPF-39. The amendment revised the 
    Technical Specification.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67858) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 16, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: November 30, 1993
        Brief description of amendments: These amendments decrease the test 
    frequency of the drywell-to-suppression chamber bypass leak test to 
    coincide with the primary Containment Integrated Leak Rate Test 
    interval and require an additional test to measure the vacuum breaker 
    leakage area for those outages for which the drywell-to-suppression 
    chamber bypass test is not scheduled.
        Date of issuance: February 17, 1994
        Effective date: February 17, 1994
        Amendment Nos. 68 and 31
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    626) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 17, 1994.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: September 28, 1992
        Brief description of amendment: The amendment revises the flow 
    requirement for the Core Spray (CS) pumps and the associated Bases. The 
    change reduces the CS pump minimum flow acceptance criteria by 10% and 
    addresses an inconsistency between the system leakage rates in the 
    Updated Final Safety Analysis Report and the Technical Specifications 
    (TS). Specifically, the surveillance testing required by the TS is 
    intended to verify the capability of a core spray pump to deliver 
    acceptable flow to the core. The new CS pump minimum flow acceptance 
    criteria now accounts for system leakage that is not delivered to the 
    core.
        Date of issuance: February 8, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 204
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 9, 1992 (57 FR 
    58250) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 8, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: April 7, 1992
        Brief description of amendments: These amendments revise Technical 
    Specifications Tables 3.3-3, 3.3-4, 3.3-5, and 4.3-2, which provide the 
    requirements for the Engineered Safety Features Actuation System 
    (ESFAS) instrumentation. This Technical Specification change will 
    clarify that a Manual Safety Injection Actuation Signal does not 
    actuate a Containment Cooling Actuation Signal. This is an editorial 
    change to make the Technical Specifications consistent with plant 
    design.
        Date of issuance: February 4, 1994
        Effective date: February 4, 1994
        Amendment Nos.: 110 and 99
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 10, 1992 (57 FR 
    24679) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 4, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: March 10, 1993; amended January 
    31, 1994 (TS 93-02)
        Brief description of amendments: The amendments add a reference to 
    the test requirements of 10 CFR 50, Appendix J, ``Primary Reactor 
    Containment Leakage Testing for Water-Cooled Power Reactors'' to the 
    technical specifications at various locations, and remove the 
    corresponding detailed test requirements and acceptance criteria. Other 
    containment system specifications related to this issue are also 
    removed. In addition, a change to Table 3.6-2, ``Containment Isolation 
    Valves,'' clarifies the additional testing requirements for the 
    containment purge valves.
        Date of issuance: February 10, 1994
        Effective date: February 10, 1994
        Amendment Nos.: 176, Unit 1 - 167, Unit 2
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: May 12, 1993 (58 FR 
    28059) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 10, 1994.No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: September 23, 1991
        Brief description of amendment: This amendment allows an alternate 
    method for verifying whether a control rod drive pump is operating.
        Date of issuance: February 14, 1994
        Effective date: February 14, 1994
        Amendment No. 55
        Facility Operating License No. NPF-58. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 13, 1991 (56 
    FR 57705) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 14, 1994. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: December 10, 1993
        Brief description of amendments: The amendments modify the 
    surveillance frequency of the Auxiliary Feedwater System pumps from 
    monthly to quarterly.
        Date of issuance: February 7, 1994
        Effective date: February 7, 1994
        Amendment Nos.:  177 and 158
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    631) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 7, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: February 23, 1993
        Brief description of amendment: The amendment revises TS Section 
    3.5, ``Instrumentation System,'' Table TS 3.5-6, ``Instrumentation 
    Operating Conditions for Indication,'' and Table TS 4.4-1, ``Minimum 
    Frequencies for Checks, Calibrations and Test of Instrument Channels.'' 
    The amendment adds operability and surveillance requirements for the 
    reactor vessel level indication and core exit thermocouple 
    instrumentation to satisfy the recommendations of Generic Letter 83-37, 
    ``NUREG-0737 Technical Specifications.'' Similar additions are made for 
    the wide range steam generator level instrumentation to satisfy 
    Regulatory Guide 1.97 recommendations. Administrative changes are also 
    incorporated as part of converting the TS document to the WordPerfect 
    software.
        Date of issuance: February 9, 1994
        Effective date: February 9, 1994
        Amendment No.: 105
        Facility Operating License No. DPR-43: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 21, 1993 (58 FR 
    39061) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 9, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: November 16, 1993, as 
    supplemented on December 7, 1993.
        Brief description of amendment: The amendment modifies KNPP TS 
    4.4.a.7 by deleting the requirement that couples the performance of the 
    Type A leakage tests to the 10-year inservice inspection program 
    requirements. This change was made to reflect the partial exemption 
    from the requirements of 10 CFR 50, Appendix J, Section III.D.a.(a), 
    which was granted by the NRC on February 14, 1994. In addition, 
    administrative changes to KNPP TS Section 4.4 and its associated bases 
    have been made.
        Date of issuance: February 17, 1994
        Effective date: February 17, 1994
        Amendment No.: 106
        Facility Operating License No. DPR-43. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67865) The December 7, 1993, submittal provided additional 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated February 17, 1994.No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: March 24, 1993
        Brief description of amendments: These amendments revised Technical 
    Specifications (TS) Section 15.6 to update several position titles, to 
    modify the composition and duties of the Manager's Supervisory Staff 
    (the onsite review committee), and to remove a redundant review of the 
    Facility Fire Protection Program implementing procedures.
        Date of issuance: January 27, 1994
        Effective date: January 27, 1994
        Amendment Nos.: 146 and 150
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 18, 1993 (58 FR 
    43940) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated January 27, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: May 27, 1993
        Brief description of amendment: The proposed changes would revise 
    the heatup, cooldown, and cold overpressure mitigation system power-
    operated relief valve setpoint pressure/temperature limits. The revised 
    limits reflect the analysis of the most recently withdrawn surveillance 
    capsule associated with the reactor vessel radiation surveillance 
    program (10 CFR 50, Appendix H). The revised limits bound operation 
    through 13.6 Effective Full Power Years (EFPY).
        Date of issuance: February 10, 1994
        Effective date: February 10, 1994, to be implemented within 30 days 
    of issuance.
        Amendment No.: 71
        Facility Operating License No. NPF-42: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36449) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated February 10, 1994.No significant 
    hazards consideration comments received: No.Local Public Document Room 
    Locations: Emporia State University, William Allen White Library, 1200 
    Commercial Street, Emporia, Kansas 66801 and Washburn University School 
    of Law Library, Topeka, Kansas 66621
        Dated at Rockville, Maryland, this 23rd day of February 1994.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Divisio Director, Division of Reactor Projects - III/IV/V, 
    Office of Nuclear Reactor Regulation
    [Doc. 94-4562 Filed 3-1-94; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
03/02/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
X94-10302
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: March 2, 1994