98-7652. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 63, Number 57 (Wednesday, March 25, 1998)]
    [Notices]
    [Pages 14482-14497]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-7652]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any
    
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    amendments issued, or proposed to be issued, under a new provision of 
    section 189 of the Act. This provision grants the Commission the 
    authority to issue and make immediately effective any amendment to an 
    operating license upon a determination by the Commission that such 
    amendment involves no significant hazards consideration, 
    notwithstanding the pendency before the Commission of a request for a 
    hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 2, 1998, through March 13, 1998. The 
    last biweekly notice was published on March 11, 1998 (63 FR 11913).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By April 24, 1998, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the
    
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    Commission may issue the amendment and make it immediately effective, 
    notwithstanding the request for a hearing. Any hearing held would take 
    place after issuance of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-325, Brunswick 
    Steam Electric Plant, Unit 1, Brunswick County, North Carolina
    
        Date of amendment request: February 23, 1998.
        Description of amendment request: The amendment request proposes 
    changes to the Brunswick Steam Electric Plant Unit 1 Technical 
    Specifications (TS) in support of Cycle 12 operation, including a 
    change to the Minimum Critical Power Ratio safety limit (safety limit 
    MCPR) to a value equivalent to the generic safety limit MCPR for 
    General Electric type GE-13 fuel. The request would additionally remove 
    a footnote limiting the stated value for the safety limit MCPR to a 
    specific fuel cycle and reference to an NRC safety evaluation 
    documenting acceptance of methods used for determining the current 
    cycle safety limit MCPR. The amendment request is provided both in the 
    format of the current TS as well as improved Standard Technical 
    Specifications (iSTS). The Brunswick licensee applied for conversion to 
    ISTS on November 1, 1996, as supplemented on October 13, 1997, and 
    February 26, 1998, and that application is currently undergoing NRC 
    staff review. For iSTS, the licensee has proposed two safety limits 
    MCPR, one pertaining to two-recirculation loop operation and the other 
    to single-recirculation loop operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed license amendment establishes a revised safety 
    limit MCPR value of 1.09 [two-recirculation loop and 1.10 for 
    single-recirculation loop operation] for use during Unit 1 Cycle 12 
    operation. General Electric (GE) has determined that both generic 
    and plant-specific evaluations [two-loop operation] yield the same 
    calculated safety limit MCPR value. Additionally, a document 
    referenced by the Technical Specification 6.9.3.2 of methodologies 
    used in determining core operating limits is being removed.
        The probability of an evaluated accident is derived from the 
    probabilities of the individual precursors to that accident. The 
    consequences of an evaluated accident are determined by the 
    operability of plant systems designed to mitigate those 
    consequences. Limits have been established, consistent with NRC[-] 
    approved methods, to ensure that fuel performance during normal, 
    transient, and accident conditions is acceptable.
        The probability of an evaluated accident is not increased by 
    revising the safety limit MCPR value to 1.09 [two-loop/1.10 single-
    loop]. The change does not require any physical plant modifications 
    or physically affect any plant components. Therefore, no individual 
    precursors of an accident are affected.
        The proposed license amendment establishes a revised safety 
    limit MCPR that ensures the fuel is protected during normal 
    operation and during any plant transients or anticipated operational 
    occurrences. Specifically, the reload analysis demonstrates that a 
    safety limit MCPR value of 1.09 [two-loop/1.10 single-loop] ensures 
    that less than 0.1 percent of the fuel rods will experience boiling 
    transition during any plant operation if the limit is not violated.
        The methods for calculating the safety limit MCPR have been 
    approved by the NRC and are described in GE's reload licensing 
    methodology topical report NEDE-24011, ``General Electric Standard 
    Application for Reactor Fuel (GESTAR II).'' Based on (1) the 
    determination of the new safety limit MCPR value using conservative 
    approved methods, and (2) the operability of plant systems designed 
    to mitigate the consequences of accidents not having been changed; 
    the consequences of an accident previously evaluated have not been 
    increased.
        Additionally, removal of the footnote on the safety limit MCPR 
    value in Technical Specification 2.1.2 and removal of reference 
    ``c'' from the document list in Technical Specification 6.9.3.2 will 
    not increase the probability or consequences of accidents previously 
    evaluated. The footnote on the safety limit MCPR value in Technical 
    Specification 2.1.2 and reference ``c'' in Technical Specification 
    6.9.3.2 were associated with the safety limit MCPR value of 1.10 for 
    Unit 1 Cycle 11 operation. Since the current safety limit MCPR value 
    of 1.10 applies only to Unit 1 Cycle 11 operation, the footnote on 
    the safety limit MCPR value in Technical Specification 2.1.2 and the 
    reference ``c'' in Technical Specification 6.9.3.2 are no longer 
    needed and should be deleted. Thus, removal of the footnote on the 
    safety limit MCPR value in Technical Specification 2.1.2 and removal 
    of reference ``c'' from Technical Specification 6.9.3.2 is an 
    administrative change that has no effect on the probability or 
    consequences of accidents previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed license amendment involves a revision of the 
    safety limit MCPR from 1.10 to 1.09 [two-loop/1.10 single-loop] 
    based on the results of both cycle-specific and generic analyses, 
    removal of the footnote on the safety limit MCPR value in Technical 
    Specification 2.1.2, and the removal of a document reference listed 
    in Technical Specification 6.9.3.2 describing the methods used only 
    during Unit 1 Cycle 11 to determine core operating limits. Creation 
    of the possibility of a new or different kind of accident would 
    require the creation of one or more new precursors of that accident. 
    New accident precursors may be created by modifications of the plant 
    configuration, including changes in allowable modes of operation. 
    This proposed license amendment does not involve any modifications 
    of the plant configuration or changes in the allowable modes of 
    operation. Therefore, no new precursors of an accident are created 
    and no new or different kinds of accidents are created.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        As previously stated, the methods for calculating the safety 
    limit MCPR have been previously approved by the NRC and are 
    described in GE's reload licensing methodology topical report NEDE-
    24011. Use of these methods ensures that the resulting safety limit 
    MCPR satisfies the fuel design safety criteria that less than 0.1 
    percent of the fuel rods experience boiling transition if the safety 
    limit is not violated. Based on the assurance that the fuel design 
    safety criteria will be met, the proposed license amendment does not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three
    
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    standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Pao-Tsin Kuo (Acting).
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: May 16, 1997.
        Description of amendment request: The proposed changes would 
    replace the existing Technical Specification (TS) 4.6.2.3 a.2 cooling 
    water flow rate of 1425 gpm with a new value of 1300 gpm.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Cooling water flow to the Containment Fan Coolers is provided by 
    the Emergency Service Water (ESW) System, and Emergency Service 
    Water is not an initiating system in any FSAR [Final Safety Analysis 
    Report] Chapter 15 analyses. Revising the minimum cooling water flow 
    to the Containment Fan Coolers will not increase the probability of 
    initiating any previously evaluated accident, because Containment 
    Fan Cooler performance and integrity will not be adversely affected. 
    The heat removal capacity of the Containment Fan Coolers will be 
    maintained consistent with the assumptions used in the existing HNP 
    [Harris Nuclear Plant] containment analyses, and, therefore, 
    containment integrity should not be challenged.
        Therefore, there would be no increase in the probability or 
    consequences of an accident previously evaluated.
        (2) The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment will not create any new accident 
    scenarios, because the change does not introduce any new single 
    failures, adverse equipment or material interactions, or release 
    paths.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        (3) The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        Although the proposed amendment replaces the TS 4.6.2.3 a.2 
    cooling water flow rate of 1425 gpm with a lower flow rate of 1300 
    gpm, a cooling water flow rate of greater than or equal to 1300 gpm 
    maintains adequate heat removal capacity as required by existing HNP 
    containment analyses. The Bases for TS 4.6.2.3 a.2 is to ensure that 
    adequate heat removal capacity is available, when the Containment 
    Fan Coolers are operated in conjunction with the Containment Spray 
    Systems, during post-LOCA [Loss-of-Coolant Accident] conditions to 
    prevent the pressure inside containment from exceeding its design 
    rating.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Pao-Tsin Kuo (Acting).
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley Power 
    Station, Unit No. 2, Shippingport, Pennsylvania
    
        Date of amendment request: October 22, 1997
        Description of amendment request: The proposed amendment would 
    modify the Technical Specifications (TSs) by reducing the reactor 
    coolant system (RCS) specific activity limits in accordance with 
    Generic Letter 95-05. The definition of DOSE EQUIVALENT I-131 would be 
    replaced with the Improved Standard TS definition wording in the first 
    sentence and an equation added based on dose conversion factors derived 
    from International Commission on Radiation Protection (ICRP) ICRP-30. 
    TS 3.4.8, Specific Activity, would be revised by reducing the DOSE 
    EQUIVALENT I-131 limit from 1.0 [micro] Ci[curies]/gram to 0.35 
    [micro]Ci[curies]/gram. Item 4.a in TS Table 4.4-12, Primary Coolant 
    Specific Activity Sample and Analysis Program, TS Figure 3.4-1, and the 
    Bases for TS 3/4.4.8 would be modified to reflect the reduced DOSE 
    EQUIVALENT I-131 limit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change reduces the reactor coolant system (RCS) 
    specific activity limits of Specification 3.4.8 from 1.0 [micro]Ci/
    gram to 0.35 [micro]Ci/gram and lowers the graph in Figure 3.4-1 by 
    39 [micro]Ci/gram following the guidance provided in Generic Letter 
    (GL) 95-05. This reduces the RCS acvitity allowed to leak to the 
    secondary side when the plant is operating so that additional margin 
    is available to support a higher allowable accident-induced leakage 
    value as justified by analysis.
        The proposed changes to Specification 3.4.8 and the definition 
    of DOSE EQUIVALENT I-131 ensure these requirements are consistent 
    with the latest analyses.
        These changes implement the more restrictive RCS activity limits 
    in accordance with applicable analyses and GL 95-05 to ensure the 
    regulations are satisfied. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not alter the configuration of the 
    plant or affect the operation with the reduced specific activity 
    limit. By reducing the specific activity limit, the limit would be 
    reached sooner to initiate evaluation of the out of limit condition. 
    The proposed changes will not result in any additional challenges to 
    the main steam system or the reactor coolant system pressure 
    boundary. Consequently, no new failure modes are introduced as a 
    result of the proposed changes. As a result, the main steam line 
    break, steam generator tube rupture and loss of coolant accident 
    analyses remain bounding. Therefore, the proposed change will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed change reduces the RCS specific activity limit to 
    0.35 [micro]Ci/gram along with lowering the Figure 3.4-1 limits by 
    39 [micro]Ci/gram. Reduction of the RCS specific activity limits 
    allows an increase in the limit for the projected SG [steam 
    generator] leakage following SG tube inspection and repair in 
    accordance with the voltage-based SG tube alternate repair criteria 
    (ARC). This follows the guidance provided in GL 95-05 and 
    effectively takes margin available in the specific activity limits 
    and applies it to the projected SG leakage for the ARC. This has 
    been determined to be an acceptable means for accepting higher
    
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    projected leakage rates while still meeting the applicable limits of 
    10 CFR [Part] 100 and GDC [General Design Criterion] 19 with respect 
    to offsite and control room doses.
        The capability for monitoring the specific activity and 
    complying with the required actions remains unchanged. In addition, 
    there is no resultant change in dose consequences. Therefore, the 
    proposed change does not involve a significant reduction in a margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: March 3, 1998.
        Description of amendment request: The licensee proposed to revise 
    Section 6.2.3.2 of the units' Technical Specifications. Currently, this 
    section prescribes that the Catawba Safety Review Group (SRG) be 
    composed of at least five individuals and at least three of these shall 
    have a bachelor's degree in engineering or related science and at least 
    2 years professional level experience in his/her field, at least 1 year 
    of which experience shall be in the nuclear field. The licensee 
    proposed to revise this section to provide the option of replacing one 
    of the three degreed individuals with one with at least 15 years of 
    professional level experience in his/her field, at least 10 years of 
    which experience shall be in the nuclear field, at least 3 years of 
    which nuclear experience shall be supervisory/managerial experience in 
    engineering, and shall hold or have held a Senior Reactor Operator 
    license. The licensee also proposed to editorially revise this section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's analysis is 
    presented below.
    
        1. Would the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No. The proposed amendment would only change administrative 
    requirements related to personnel qualifications for one of the five 
    SRG [Safety Review Group] positions. The SRG is an oversight group, 
    and the individual who meets the new qualification requirements 
    would be expected to perform at the same level of quality as an 
    individual who meets the current qualification requirements. 
    Changing qualification requirements for an individual who primarily 
    performs an oversight function will not have any direct effect on 
    the design or operation of any plant structures, systems, or 
    components. No previously analyzed accidents were initiated by the 
    functions of the SRG, and the SRG was not a factor in the 
    consequences of previously analyzed accidents. Therefore, the 
    proposed change would have no impact on the consequences or 
    probabilities of any previously evaluated accidents.
        2. Would the change create the possibility of a new or 
    difference kind of accident from any accident previously evaluated?
        No. The proposed change would not lead to any hardware or 
    operating procedure change. Hence, no new equipment failure modes or 
    accidents from those previously evaluated will be created.
        3. Would the change involve a significant reduction in a margin 
    of safety?
        No. Margin of safety is associated with confidence in the design 
    and operation of the plant. The proposed change to the Technical 
    Specifications does not involve any change to plant design or 
    operation. Thus, the margin of safety previously analyzed and 
    evaluated is maintained.
    
        Based on this analysis, it appears that the three standards of 10 
    CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
        Attorney for licensee: Mr. Paul R. Newton, Legal Department 
    (PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte, 
    North Carolina.
        NRC Project Director: Herbert N. Berkow.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: February 7, 1997.
        Description of amendment request: The proposed amendment, if 
    approved, would revise Technical Specification (TS) as delineated 
    below:
        1. 4160 Volt Tie From Unit 2.
        TS sections 3.7.2.b & d to delete reference to the optional use of 
    the 4160 volt tie from the unit 2 transformer.
        2. Emergency Load Sequence and Power Transfer.
        a. The testing required by Section 4.5.1.1.b of the TS would be 
    considered satisfactory if the pumps have started and valves have 
    completed travel. The need to evidence the successful starting of pumps 
    and fans and the complete travel of valves by observation of control 
    board component operating lights will be deleted. Neither would a 
    second means of verification, such as: the station computer or control 
    board indicating lights initiated by separate limit switch contacts be 
    required.
        b. Section 4.5.1.2.b would be revised in the same manner as 
    4.5.1.1.b above.
        3. Reactor Building Cooling and Isolation System.
        a. Section 4.5.3.1.a.1 of the TS would be revised to delete the 
    need to simultaneously test start a spray pump using a Reactor Building 
    30-psi high pressure test signal while testing the emergency loading 
    sequence.
        The proposed change also eliminates the need to evidence the 
    successful starting of the spray pumps by observation of the control 
    board indicating lights or the use of the station computer for Sections 
    4.5.3.1.a.1 and 4.5.3.1.b.2.
        4. Instrument Surveillance Requirements.
        Table 4.1-1 of the TS would be revised to delete the strong motion 
    accelerometer and its quarterly battery check surveillance requirement.
        5. Air Intake Tunnel (AIT) Fire Protection Systems.
        Section 5.5 of the TS would be deleted. The description of the 
    equipment contained in Section 5.5 would be transferred to the Final 
    Safety Analysis Report (FSAR).
        6. Hydrogen Recombiner System.
        The Bases for Section 4.4.4 TS would be changed to reflect a 
    reduction in the time interval for operation of the hydrogen recombiner 
    following a loss of cooling accident (LOCA) from 9.8 to 9 days.
        7. Various editorial and typographical errors would be corrected.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated. The revised TS eliminate overly prescriptive 
    requirements for evidencing component performance, the requirement 
    for redundant diesel block loading tests,
    
    [[Page 14487]]
    
    instrumentation from SR [surveillance requirement] tables having no 
    associated LCO [limiting condition for operation], AIT fire 
    protection systems descriptive text, and correct previous 
    typographical errors. Several of the proposed revisions involve 
    changes which are consistent with NUREG-1430, the Revised Standard 
    Technical Specifications (RSTS) for B&W plants. The reliability of 
    systems and components depended upon to prevent or mitigate the 
    consequences of accidents previously evaluated is not degraded by 
    the proposed changes because assurance of system and equipment 
    availability is maintained by surveillance testing program 
    requirements.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The revised 
    surveillance requirements create no new failure modes. Verification 
    of equipment operation continues to be required by plant procedures. 
    Elimination of the AIT fire protection system descriptive text from 
    the TSs would not create a new or different kind of accident since 
    the change has no effect on surveillance methodology and frequency 
    requirements. They are maintained in the Fire Protection Program.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety because no operating limits are affected.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Cecil O. Thomas, Director.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of amendment request: March 3, 1998.
        Description of amendment request: The proposed revision to the 
    Millstone Unit 3 licensing basis would eliminate the requirement to 
    have the recirculation spray system directly inject into the reactor 
    coolant system following a design basis accident.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Northeast Nuclear Energy Company (NNECO) has reviewed the 
    proposed revision in accordance with 10CFR50.92 and has concluded 
    that the revision does not involve a significant hazards 
    consideration (SHC). The basis for this conclusion is that the three 
    criteria of 10CFR50.92(c) are not satisfied. The proposed revision 
    does not involve an SHC because the revision would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The change to the Emergency Operating Procedures (EOP) to 
    eliminate the use of Recirculation Spray System (RSS) direct 
    injection during cold and hot leg recirculation does not effect the 
    probability of any accident. The elimination of the requirement to 
    have RSS directly [inject] into the reactor coolant system did not 
    increase the consequences of the previously evaluated accidents. 
    These consequences were evaluated based on very conservative 
    assumptions concerning the containment pressure after the design 
    basis Loss of Coolant Accident (LOCA), containment integrated 
    leakage rates, and the fraction of the sprayed volume. None of these 
    assumptions were affected by the elimination of the direct cold-leg 
    injection.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The modification to the RSS did not create the possibility of a 
    new or different accident from those previously analyzed. The change 
    involved elimination of the direct injection flow path from the 
    design basis of the system but did not involve physical 
    modifications to the system itself. The operability of the affected 
    valves within the direct injection alignments remained unchanged and 
    these paths were still available to the operators for contingencies 
    beyond the design basis. The EOPs provided clear and explicit 
    guidance to that effect.
        Therefore, the proposed revision does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        In considering the impact on the margin of safety as defined in 
    the bases of the Technical Specifications, the impact of the change 
    on the design basis analysis of the fission product barriers must be 
    evaluated.
        The minimum Emergency Core Cooling System flow requirement for 
    long-term core cooling is that the modified alignment deliver 
    sufficient flow to satisfy the inventory lost to the boil off in the 
    vessel due to the decay heat and the extended boiling from hot metal 
    in the downcomer and the lower plenum. The analysis determined that 
    these requirements were being met.
        The elimination of the direct injection resulted in a flow 
    reduction through the RSS heat exchanger, from approximately 4000 
    gpm [gallons per minute] to 1200 gpm, thus reducing the rate of the 
    heat transfer from the containment to the service water system. The 
    design basis of the containment heat removal systems (circa 1986) is 
    that the containment pressure will decrease to subatmospheric within 
    one hour after the Design Basis Accident to compensate for the 
    reduction in heat removal from the containment, a smaller allowable 
    RSS pump degradation was assumed in the revised containment 
    analysis. The original RSS pump performance curve was based on a 10 
    percent reduction in developed head from the design curve. For the 
    modification, a 5 percent reduction was used. The results of the 
    analysis show that with these changes the design basis of 
    maintaining subatmospheric containment pressure was met.
        Based on the above, elimination of the direct injection did not 
    reduce the margin of safety because there was no violation of the 
    acceptance limits and no weakening of the protective boundaries.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    Connecticut.
        NRC Deputy Director: Phillip F. McKee.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of amendment requests: November 2, 1995, as supplemented by 
    letter dated January 9, 1998. The January 9, 1998, submittal supersedes 
    the staff's proposed no significant hazards consideration determination 
    evaluation for the requested changes that was published on April 10, 
    1996 (61 FR 15995).
        Description of amendment requests: In the November 2, 1995, letter, 
    the
    
    [[Page 14488]]
    
    licensee proposed to revise Technical Specification (TS) 3.8.1, ``AC 
    Sources--Operating,'' to extend the offsite circuit completion time and 
    to extend the allowed outage time for an emergency diesel generator. 
    The January 9, 1998, letter modifies the original request to (1) 
    further extend the offsite completion time and allowed outage time for 
    an emergency diesel generator, and (2) add a new TS 5.5.2.14, 
    ``Configuration Risk Management Program,'' that ensures a 
    proceduralized probabilistic risk assessment-informed process is in 
    place that assesses the overall impact of plant maintenance on plant 
    risk.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Emergency Diesel Generators (EDGs) are backup alternating 
    current power sources design to power essential safety systems in 
    the event of a loss of offsite power. EDGs are not accident 
    initiators in any accident previously evaluated. Therefore, this 
    change does not involve an increase in the probability of an 
    accident previously evaluated.
        The EDGs provide backup power to components that mitigate the 
    consequences of accidents. The proposed changes to the Completion 
    Times do not affect any of the assumptions used in the deterministic 
    safety analysis.
        To fully evaluate the effect of the EDG Completion Time 
    extension, Probabilistic Safety Analysis (PSA) methods were 
    utilized. The results of these analyses show no significant increase 
    in the core damage frequency. As a result, there would be no 
    significant increase in the consequences of accidents previously 
    evaluated.
        The Configuration Risk Management Program is an Administrative 
    Program that assesses risk based on plant status. Adding the 
    requirement to implement this program for Technical Specification 
    3.8.1 does not affect the probability or the consequences of an 
    accident.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This proposed change does not alter the design, configuration, 
    or method of operation of the plant. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect the Limiting Conditions for 
    Operation or their Bases that are used in the deterministic analyses 
    to establish the margin of safety. PSA evaluations were used to 
    evaluate these changes and these evaluations determined that the 
    changes are either risk neutral or risk beneficial.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of amendment requests: December 19, 1997.
        Description of amendment requests: The licensee proposed to revise 
    Technical Specification (TS) 3.4.9, ``Pressurizer,'' to reduce the 
    allowable pressurizer water volume for pressurizer operability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The limiting events impacted by this Technical Specification 
    change have been reanalyzed. These events are the Chemical and 
    Volume Control System (CVCS) Malfunction and CVCS Malfunction With a 
    Concurrent Single Failure of an Active Component, Inadvertent 
    Operation of the Emergency Core Cooling System (ECCS) During Power 
    Operation (Including Single Failure of an Active Component), and 
    Feedwater System Pipe Breaks. The probability of these events is not 
    changed by the restriction of the pressurizer level to 57%. An 
    operator action time of 15 minutes has been identified for the CVCS 
    malfunction and inadvertent ECCS operation events. Based on the 
    availability of operator alarms and indications and operator 
    Simulator training, 15 minute operator action is sufficient to 
    recognize and mitigate the inadvertent CVCS or ECCS operation. 
    Therefore, this change will not involve an increase in the 
    probability or consequences of any previously evaluated accident.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This amendment request does not involve any change to plant 
    equipment or operation. All the events identified in Chapter 15 of 
    the Updated Final Safety Analysis Report (UFSAR) were evaluated to 
    determine the impact of the change in pressurizer level. In addition 
    to the normally analyzed Inadvertent Operation of the ECCS During 
    Power Operation event a concurrent single failure of an active 
    component was considered in this evaluation. The analysis of this 
    event with single failure of an active component produced 
    consequences that are bounded by the CVCS malfunction with single 
    failure of an active component. No new or different kind of accident 
    will be created as a result of this Technical Specification change. 
    Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        This amendment request does not change the manner in which 
    safety limits, limiting safety settings, or limiting conditions for 
    operation are determined. There are no changes to the acceptance 
    criteria for these events as a result of the proposed reduction in 
    the maximum pressurizer water level. This change does not reduce a 
    margin of safety since it lowers allowed pressurizer operational 
    level to 57%. An operator action time of 15 minutes has been 
    identified for the CVCS malfunction and inadvertent ECCS operation 
    events. Based on the availability of operator alarms and 
    indications, and demonstrated operator response in Simulator 
    training, 15 minute operator action has been demonstrated to be 
    adequate to recognize and mitigate the inadvertent CVCS or ECCS 
    operation. Therefore, this proposed change does not involve a 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    [[Page 14489]]
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of amendment requests: January 2, 1998.
        Description of amendment requests: The licensee proposed to revise 
    Technical Specification (TS) 3.7.5, ``Auxiliary Feedwater (AFW) 
    System,'' to indicate the turbine driven AFW pump is operable when 
    running in the manual mode to support plant startups, shutdowns, and 
    testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Probabilistic analyses have been performed in support of 
    declaring P140 operable when the pump is manually actuated and 
    operating.
        The results show that, considering P-140 to be in test for an 
    entire year, the core damage risk of a Main Steam Line Break/
    Feedwater Line Break (MSLB/FWLB) slightly increases (4.3E-8/yr) 
    while the risk due to other initiating events decreases (3E-7/yr). 
    The net core damage impact of P-140 in test for an entire year is a 
    Core Damage Frequency (CDF) decrease of 2E-7/yr. Having P140 
    operating instead of being in standby increases its reliability. 
    This increased reliability reduces the risk due to other initiating 
    events, such as loss of main feedwater, medium and small Loss of 
    Coolant Accidents (LOCAs), Steam Generator Tube Rupture (SGTR), and 
    Loss of Offsite Power (LOP), which require Auxiliary Feedwater (AFW) 
    and which occur with much greater frequency than MSLB/FWLB. With the 
    overall CDF reduction a result of considering P140 being in a test 
    configuration for an entire year, the actual cumulative risk 
    incurred is the weighted fraction that P140 is in the test 
    configuration over a year period. Based on past experience, the pump 
    is running in manual approximately 500 minutes/year, which results 
    in an annual net cumulative CDF reduction on the order of 2E-10/yr 
    due to running P140 in the manual mode.
        Therefore, the operation of the facility in accordance with this 
    proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This change does not involve a plant hardware modification or 
    allow the operation of any plant equipment in any way other than 
    originally designed. This change only affects the administrative 
    tracking of the turbine-driven AFW pump when the steam driven AFW 
    pump is operating in the manual mode.
        Therefore, the operation of the facility in accordance with this 
    proposed change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Pump history shows the pump is run approximately 500 minutes per 
    year. In all cases except for the one postulated scenario of the 
    Main Steam Isolation Signal followed by an Emergency Feedwater 
    Actuation Signal the turbine-driven AFW pump is not susceptible to 
    being tripped. Also, this postulated scenario does not affect the 
    capability of the motor-driven AFW pumps.
        Even though there is a small increase in the CDF from the AFW 
    steam driven pump operating in manual mode based on the possibility 
    of a MSLB/FWLB, also considering other initiating events results in 
    an annual net cumulative CDF reduction on the order of 2E-10/yr due 
    to P140 running in the manual mode.
        Therefore, the operation of the facility in accordance with this 
    proposed change does not involve a significant reduction in the 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear
    
        Date of amendment request: August 20, 1997, as supplemented by 
    letters dated September 18, 1997 and October 31, 1997.
        Description of amendment request: The proposed change would revise 
    the Vermont Yankee Technical Specifications Section 6.0, 
    ``Administrative Controls,'' to add and revise reference to NRC-
    approved methodologies which will be used to generate the cycle-
    specific thermal operating limits in the Vermont Yankee Core Operating 
    Limits Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change will not involve any significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The change updates the Technical Specifications to include an 
    NRC approved method reference to allow calculation of thermal limits 
    with a revised method. It does not affect plant operation and will 
    not weaken or degrade the facility.
        2. The proposed change will not create the possibility of a new 
    or different kind of accident since the change is administrative. No 
    physical alterations of the plant, setpoint changes, or operating 
    conditions are proposed.
        3. The proposed change will not involve a significant reduction 
    in a margin of safety. The change involves an update to the 
    Administrative Controls in Section 6.0 of the Technical 
    Specifications by adding a reference to NRC approved methods. This 
    administrative change does not alter plant safety margins.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, N.W., Washington, DC 20037-1128.
        NRC Project Director: Cecil O. Thomas, Director.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: February 4, 1998.
        Description of amendment request: The amendment would revise 
    Technical Specification 3.2.4, quadrant power tilt ratio (QPTR), and 
    associated Bases, to clarify the required actions for the limiting 
    condition for operation (LCO) and other changes consistent with the 
    technical specification conversion application submitted by letter 
    dated May 15, 1997.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
    
    [[Page 14490]]
    
    1. Requirements for Determining QPTR
    
        The Action to calculate QPTR once per hour until THERMAL POWER 
    was reduced to less than 50% RATED THERMAL POWER (RTP) when QPTR 
    exceeds the LCO requirements would be deleted and replaced by a new 
    requirement to determine QPTR at least once per 12 hours.
        The proposed change involves only the compensatory measures to 
    be taken should the QPTR be outside its limit. The frequency with 
    which QPTR is calculated is not assumed in the initiating events for 
    any accident previously evaluated. In addition, the change does not 
    involve any new operating activities or hardware change. Therefore, 
    the proposed change would not significantly increase the probability 
    of an accident previously evaluated.
        Once THERMAL POWER has been reduced appropriately in proportion 
    to the amount that QPTR exceeds 1.00, any additional change would be 
    sufficiently slow that a 12-hour interval for recalculating QPTR 
    will provide an adequate level of protection. Therefore, the 
    proposed change will not significantly increase the consequences of 
    any accident previously evaluated.
    
    2. Completion Time for Resetting the Power Range Neutron Flux-High Trip 
    Setpoints
    
        The proposed change to allow 72 hours for resetting the Power 
    Range Neutron Flux-High trip setpoints involves only the 
    compensatory measures to be taken should the QPTR be outside its 
    limit. These compensatory measures are not assumed in the initiating 
    events for any accident previously evaluated. The proposed actions 
    recognize that the required reduction in power (3% for each 1% of 
    indicated QPTR in excess of 1.00) provide adequate margin for fuel 
    design limits so that consequences of assumed accidents would not be 
    significantly affected. Therefore, the proposed change will not 
    adversely affect the probability or consequences of any accident 
    previously evaluated. Further, by permitting more time to perform 
    resetting the trip setpoints, the chances of a transient may be 
    reduced.
    
    3. Delete(tion) of the Actions (a.3., a.4.) for verifying QPTR to be 
    restored within 24 hours and for identifying and correcting the cause 
    of the out-of-limit condition prior to increasing THERMAL POWER
    
        The proposed changes would delete current Actions a.3. and a.4. 
    and add new Actions for QPTR out of limit including requirements for 
    measuring FQ(Z) and F N delta H prior to and 
    following a return to power and performing safety analyses to verify 
    safety requirements are met prior to increasing power above the 
    limits of Action a.1. The proposed changes involve only the 
    compensatory measures to be taken should the QPTR be outside its 
    limit. These compensatory measures are not assumed in the initiating 
    events for any accident previously evaluated. Therefore, the 
    proposed change will not affect the probability or consequences of 
    any accident previously evaluated.
    
    4. Deletion of the Actions for QPTR in excess of 1.09
    
        The proposed change would delete the required Actions for QPTR 
    in excess of 1.09 and Actions for QPTR in excess of 1.02 are 
    followed for all instances where QPTR exceeds 1.02. The proposed 
    change involves only the compensatory measures to be taken should 
    the QPTR be outside its limit. These compensatory measures are not 
    assumed in the initiating events for any accident previously 
    evaluated. The proposed actions recognize that the required 
    reduction in power (3% for each 1% of indicated QPTR in excess of 
    1.00) provide adequate margin for fuel design limits so that 
    consequences of assumed accidents would not be significantly 
    affected. Therefore, the proposed change will not affect the 
    probability or consequences of any accident previously analyzed.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
    
    1. Requirements for Determining QPTR
    
        The proposed change for calculating QPTR once every 12 hours 
    does not involve a physical alteration to the plant or change the 
    method by which any safety-related system performs its function. The 
    manner in which the plant would be operated would not be altered. 
    Therefore, the proposed change will not create the possibility of a 
    new or different kind of accident from any previously evaluated.
    
    2. Completion Time for Resetting the Power Range Neutron Flux-High Trip 
    Setpoints
    
        The proposed change to allow 72 hours for resetting the Power 
    Range Neutron Flux-High trip setpoints does not involve a permanent 
    physical alteration to the plant; no new or different kinds of 
    equipment will be installed. The change would not alter the manner 
    in which the plant would be operated only the timing of actions that 
    provide potential mitigation of accidents. Thus, the change would 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
    
    3. Delete the Actions (a.3., a.4.) for verifying QPTR to be restored 
    within 24 hours and for identifying and correcting the cause of the 
    out-of-limit condition prior to increasing THERMAL POWER
    
        The proposed changes would delete current Actions a.3, and a.4. 
    and add new Actions for QPTR out-of-limit including requirements for 
    measuring FQ(Z) and F N delta H prior to and 
    following a return to power and performing safety analyses to verify 
    safety requirements are met prior to increasing power above the 
    limits of Action a.1. The proposed changes do not involve a physical 
    alteration to the plant; no new or different kinds of equipment 
    would be installed. The changes would not alter the manner in which 
    the plant would be operated only the timing of actions that provide 
    potential mitigation of accidents. Thus, the changes would not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
    
    4. Deletion of the Actions for QPTR in excess of 1.09
    
        The proposed change would delete the required Actions for QPTR 
    in excess of 1.09 and Actions for QPTR in excess of 1.02 are 
    followed for all instances where QPTR exceeds 1.02. The proposed 
    change does not involve a physical alteration to the plant or 
    changes in the way in which the plant is operated. The proposed 
    change involves only the compensatory measures to be taken should 
    QPTR be outside its limit. The assumptions of the accident analyses 
    are unaffected by the proposed change. No new permutations or event 
    initiators are introduced by the proposed alternate methods of 
    dealing with QPTRs in excess of 1.09. Therefore, there is no 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
    
    1. Requirements for Determining QPTR
    
        The proposed change for calculating QPTR once every 12 hours 
    does not change any accident analysis assumptions, initial 
    conditions or results. The proposed change will continue to ensure 
    that the plant is maintained in a safe condition while QPTR is in 
    excess of its limit. Additionally, calculating QPTR once per 12 
    hours as opposed to every hour while QPTR is in excess of its limit 
    would avoid the diversion of personnel resources from corrective 
    actions with regard to meeting the LCO. Therefore, the proposed 
    change will not involve a significant reduction in any margin of 
    safety.
    
    2. Completion Time for Resetting the Power Range Neutron Flux-High Trip 
    Setpoints
    
        The proposed change to allow 72 hours for resetting the Power 
    Range Neutron Flux-High trip setpoints will continue to ensure that 
    the plant is maintained in a safe condition within the envelope of 
    the safety analyses while QPTR is in excess of its limit. The 
    proposed actions recognize that the required reduction in power (3% 
    for each 1% of indicated QPTR in excess of 1.00) provide adequate 
    margin for fuel design limits so that consequences of assumed 
    accidents would not be significantly affected. Therefore, the 
    proposed change will not involve a significant reduction in any 
    margin of safety.
    
    3. Delete the Actions (a.3., a.4.) for verifying QPTR to be restored 
    within 24 hours and for identifying and correcting the cause of the 
    out-of-limit condition prior to increasing THERMAL POWER
    
        The proposed changes would delete current Actions a.3. and a.4 
    and add new Actions for QPTR out-of-limit including requirements for 
    measuring FQ(Z) and F N delta H prior to and 
    following a return to power and performing safety analyses to verify 
    safety requirements are met prior to increasing power above the 
    limits of Action a.1. The proposed changes will continue to ensure 
    that the plant is maintained in a safe condition within the envelope 
    of the safety analysis while QPTR is in excess of its limit. 
    Therefore, the proposed changes will not involve a significant 
    reduction in any margin of safety.
    
    4. Deletion of the Actions for QPTR in excess of 1.09
    
        The proposed change would delete the required Actions for QPTR 
    in excess of 1.09
    
    [[Page 14491]]
    
    and Action for QPTR in excess of 1.02 are followed for all instances 
    where QPTR exceeds 1.02. The proposed change will continue to ensure 
    that the plant is maintained in a safe condition within the envelope 
    of the safety analyses while QPTR is in excess of its limit. While 
    different actions are taken in response to a QPTR in excess of 1.09, 
    the proposed change will assure that accident analyses assumptions 
    continue to be met. Therefore, the proposed changes will not involve 
    a significant reduction in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037.
        NRC Project Director: William H. Bateman.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: February 4, 1998.
        Description of amendment request: The amendment would revise the 
    technical specifications to (1) create separate functional units for 
    the analog and digital portions of the engineered safety features 
    actuation system (ESFAS) function associated with starting the turbine-
    driven auxiliary feedwater pump on a loss of offsite power, and (2) add 
    a table notation to clarify that the testing of the time delay relays 
    for the 4 kV undervoltage, loss of voltage and grid degraded voltage 
    portion of the ESFAS is performed as part of the channel calibration.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Overall protection system performance will remain within the 
    bounds of the previously performed accident analyses since no 
    hardware changes are proposed. The recognition that different 
    OPERABILITY and surveillance requirements apply to analog vs. 
    digital circuitry does not impact any previously analyzed accidents. 
    The clarification that testing of the time delay relays is performed 
    as part of the CHANNEL CALIBRATION does not impact any previously 
    analyzed events. The proposed change will not affect any of the 
    analysis assumptions for any of the accidents previously evaluated. 
    The proposed change does not alter the current method or procedures 
    for meeting the surveillance requirements in Table 4.3-2. The 
    proposed change will not affect the probability of any event 
    initiators nor will the proposed change affect the ability of any 
    safety-related equipment to perform its intended function. There 
    will be no degradation in the performance of nor an increase in the 
    number of challenges imposed on safety-related equipment assumed to 
    function during an accident situation. Therefore, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There are no hardware changes nor are there any changes in the 
    method by which any safety-related plant system performs its safety 
    function. The separation of analog and digital portions of 
    Functional Unit 6.f or the clarification of testing of the time 
    delay relays will not impact the normal method of plant operation.
        The OPERABILITY requirements, ACTION Statement, and surveillance 
    requirements for the analog portion, new Functional Unit 6.f.1), are 
    identical to those of Functional Unit 8.a, while the requirements 
    for the digital portion, new Functional Unit 6.f.2), are consistent 
    with the current technical specifications, other than the new ACTION 
    Statement 30 provisions that defer to the TDAFW pump Specification 
    3.7.1.2 requirements and the performance of a TADOT during 
    appropriate plant conditions. These changes do not change any ESFAS 
    design standard and are appropriate for digital functions such as 
    this.
        Testing of the time delay relays has been performed as part of 
    the 18 month CHANNEL CALIBRATION. The tolerancesfor the time delay 
    relays are sufficient to account for relay drift encountered during 
    the 18 month surveillance testing. The calculated tolerances for the 
    time delay setpoints have been evaluated to insure that safety-
    related systems, subsystems and components would not be adversely 
    affect[ed] by the drift within the permissible tolerance band.
        No new accident scenarios, transient precursors, failure 
    mechanisms, or limiting single failures are introduced as a result 
    of this change. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not affect the acceptance criteria for 
    any analyzed event. There will be no effect on the manner in which 
    safety limits or limiting safety system settings are determined nor 
    will there be any effect on those plant systems necessary to assure 
    the accomplishment of protection functions. There will be no impact 
    on any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037.
        NRC Project Director: William H. Bateman.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments toFacility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: January 26, 1998.
        Brief description of amendment request: The proposed amendment 
    would change the SSES Technical Specifications facility staff 
    requirements to allow an individual who does not hold a current senior 
    reactor operator (SRO) license to hold the position of Manager-Nuclear 
    Operations (MNO) and require an individual serving in the capacity of 
    the Operations Supervisor-Nuclear to hold a current SRO license
    
    [[Page 14492]]
    
    and report directly to the MNO and be responsible for directing the 
    licensed activities of licensed operators.
        Date of publication of individual notice in Federal Register: 
    February 24, 1998 (63 FR 9270).
        Expiration date of individual notice: March 26, 1998.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: February 25, 1998, TXX-98050.
        Description of amendment request: The proposed amendment would be a 
    temporary change to the Technical Specifications to remove the 
    requirement to demonstrate the load shedding feature of MCC XEB4-3 as 
    part of Surveillance Requirements (SRs) 4.8.1.1.2f.4)a) and 
    4.8.1.1.2f.6)a) until the plant startup subsequent to the next 
    refueling outage or until an outage of greater than 24 hours in 
    duration for each respective unit. This temporary change is requested 
    as a result of the failure to confirm the load shedding feature of MCC 
    XEB4-3 during the last performance of these SRs for the Unit 1 and Unit 
    2 train B diesel generators (DGs).
        Date of individual notice in the Federal Register: March 9, 1998, 
    (63 FR 11458).
        Expiration date of individual notice: April 8, 1998.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: March 18, 1997, as supplemented 
    by letters dated July 28, 1997, and September 9, 1997.
        Brief description of amendments: The amendments revise the 
    operating licenses to reflect approval of Amendment 42 to the Palo 
    Verde Nuclear Generating Station Physical Security Plan. The amendments 
    revise the methods used to search materials, packages, and personnel 
    prior to their entry into the protected area, as described in the 
    security plan.
        Date of issuance: March 4, 1998.
        Effective date: March 4, 1998.
        Amendment No.: Unit 1-115; Unit 2-108; Unit 3-87.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the operating licenses.
        Date of initial notice in Federal Register: October 8, 1997 (62 FR 
    52580).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 4, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: December 17, 1997, as 
    supplemented by letters dated February 6, 1998 and March 12, 1998.
        Brief description of amendment: The proposed change would revise 
    Technical Specifications Section 5.6.5, ``Core Operating Limits 
    Report.'' The revisions add reference to an additional approved 
    methodology for correlating departure from nucleate boiling (DNB) 
    ratios. The added methodology is the Siemens Power Corporation Topical 
    Report, EMF-92-153(P)(A), ``HTP: Departure from Nucleate Boiling 
    Correlation for High Thermal Performance Fuel.''
        Date of issuance: March 16, 1998.
        Effective date: March 16, 1998.
        Amendment No. 178.
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4309). The February 6 and March 12, 1998 submittals provided clarifying 
    information that did not affect the initial determination of no 
    significant hazards considerations. The Commission's related evaluation 
    of the amendment is contained in a Safety Evaluation dated March 16, 
    1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois, Docket 
    Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 1 and 
    2, Rock Island County, Illinois
    
        Date of application for amendments: October 27, 1997.
        Brief description of amendments: The amendments would change the 
    Dresden and Quad Cities Technical Specifications (TS) to clarify the 
    applicability, action and surveillance requirements for the Standby 
    Liquid Control System (SLCS). The changes would make the current TS 
    requirements for the SLCS consistent with the Improved Standard 
    Technical Specifications (ISTS) contained in NUREG-1433, ``Standard 
    Technical Specifications General Electric Plants, BWR/4.''
        Date of issuance: March 6, 1998.
    
    [[Page 14493]]
    
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 167, 162, and 180, 178.
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 14, 1998 (63 FR 
    2277).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 6, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: October 2, 1996, as supplemented 
    July 31, 1997.
        Brief description of amendment: The amendment revises Figures 
    3.1.A-1, 3.1.A-2 and 3.1.A-3, Section 3.1.B and its Bases, Figures 
    3.1.B-1 and 3.1.B-2, and the Bases of Section 4.3 and Figure 4.3-1 of 
    the Technical Specifications to incorporate the revised Indian Point 
    Unit 2 Heatup and Cooldown Limit Curves for Normal Operation.
        Date of issuance: February 27, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 195.
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 19, 1996 (61 
    FR 58901).
        The July 31, 1997, letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 27, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: December 17, 1997Brief 
    description of amendments: The amendments revise Section 6.9.1.9 of the 
    Technical Specifications to reference updated or recently approved 
    topical reports, which contain methodologies used to calculate cycle-
    specific limits contained in the Core Operating Limits Report.
        Date of issuance: March 2, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1-163; Unit 2-155.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4310).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of application for amendment: July 21, 1997, as supplemented 
    February 18, 1998.
        Brief description of amendment: Technical Specification Change 
    Request concerning Emergency Feedwater Surveillance Testing. This 
    request is to make several changes to the ANO-2 Technical 
    Specifications including extension of the emergency feedwater (EFW) 
    pump surveillance testing frequency, a reduction in the minimum steam 
    generator pressure required to perform the surveillance testing on the 
    turbine-driven EFW pump, and a modification to the EFW pump testing 
    requirements.
        Date of issuance: March 12, 1998.
        Effective date: March 12, 1998.
        Amendment No.: 188.
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications/license.
        Date of initial notice in Federal Register: August 13, 1997 (62 FR 
    43367).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 12, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of application for amendment: September 23, 1997, as 
    supplemented by letters dated February 27 and March 4, 1998.
        Brief description of amendment: The amendment changes the Reactor 
    Protective System (RPS) and Engineering Safety Actuation System (ESFAS) 
    trip set point and allowable values for steam generator low pressure. 
    The amendment also relocates the RPS and ESFAS response time tables 
    from the Technical Specifications to the Safety Analysis Report as 
    described in NRC Generic Letter 93-08, ``Relocation of Technical 
    Specification Tables of Instrument Response Time Limits,'' dated 
    December 29, 1993.
        Date of issuance: March 12, 1998.
        Effective date: March 12, 1998.
        Amendment No.: 189.
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications/license.
        Date of initial notice in Federal Register: January 28, 1998, (63 
    FR 4311).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 12, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of application for amendment: September 23, 1997, as 
    supplemented by letters dated February 27 and March 4, 1998.
        Brief description of amendment: The amendment reduces the minimum 
    required reactor coolant system flow rate in TS 3.2.5 until the ANO-2 
    steam generators are replaced. The reduced reactor coolant system flow 
    requirement will account for plugging of up to approximately 30 percent 
    of the tubes in the existing steam generators at ANO-2.
        Date of issuance: March 12, 1998.
        Effective date: March 12, 1998.
        Amendment No.: 190.
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications/license.
        Date of initial notice in Federal Register: January 28, 1998, (63 
    FR 4312).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 12, 1998.
    
    [[Page 14494]]
    
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Unit No. 3 Nuclear Generating Plant, Citrus County, Florida
    
        Date of application for amendment: December 5, 1997, as 
    supplemented December 11, 1997, January 9, February 12 and 19, 1998.
        Brief description of amendment: To revise the Final Safety Analysis 
    Report (FSAR) and the Improved Technical Specification Bases to reflect 
    the modified reactor building fan recirculation system fan cooler 
    starting logic.
        Date of issuance: March 9, 1998.
        Effective date: March 9, 1998.
        Amendment No.: 165.
        Facility Operating License No. DPR-31: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 15, 1998 (63 FR 
    2423). The supplemental letters dated December 11, 1997, January 9, 
    February 12 and 19, 1998, did not change the original no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 9, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida.
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC-A5A, P.O. Box 14042, St. Petersburg, Florida 
    33733-4042.
        NRC Project Director: Frederick J. Hebdon.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of application for amendments: May 14, 1997, as supplemented 
    by letter dated October 9, 1997 (published in Federal Register as May 
    15, 1997).
        Brief description of amendments: The amendments revised the 
    combined Technical Specifications (TS) for the Diablo Canyon Power 
    Plant (DCPP) Unit Nos. 1 and 2 to revise the surveillance frequencies 
    from at least once every 18 months to at least once per refueling 
    interval (nominally 24 months) including (1) reactor coolant system 
    total flow rate, (2) instrumentation for radiation monitoring, (3) 
    instrumentation and controls for remote shutdown, (4) instrumentation 
    for accident monitoring, and (5) several miscellaneous TS.
        Date of issuance: February 27, 1998.
        Effective date: February 27, 1998, to be implemented within 90 days 
    of the date of issuance.
        Amendment Nos.: Unit 1-123; Unit 2-121.
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 30, 1997 (62 FR 
    40855).
        The October 9, 1997, supplemental letter provided additional 
    clarifying information and did not change the staff's initial no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 27, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: January 2, 1997, as supplemented 
    November 13, 1997.
        Brief description of amendment: The amendment changes the Technical 
    Specifications by extending the surveillance interval for the 
    functional testing of certain Inservice Inspection American Society of 
    Mechanical Engineers Code Class 1, 2, and 3 pumps and valves from once 
    a month to once a quarter.
        Date of issuance: March 2, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 178.
        Facility Operating License No. DPR-64: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14468).
        The November 13, 1997, submittal contained clarifying information 
    that did not change the staff's proposed finding of no significant 
    hazards consideration.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: December 14, 1995, as 
    supplemented September 26, 1997.
        Brief description of amendment: The amendment changes the James A. 
    FitzPatrick Technical Specifications (TSs) to incorporate the inservice 
    testing requirements of Section XI of the American Society of 
    Mechanical Engineers Boiler and Pressure Vessel Code. The amendment 
    supplements Amendment No. 241, dated December 2, 1997, by issuing seven 
    TS pages inadvertently omitted from Amendment No. 241.
        Date of issuance: February 27, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 242.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1635).
        The September 26, 1997, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated February 27, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: December 15, 1997.
        Brief description of amendments: The amendments revise the 
    Technical Specifications (TSs) to adopt Option B, of 10 CFR Part 50, 
    Appendix J, ``Primary Reactor Containment Leakage Testing for Water-
    Cooled Power Reactors,'' to implement a performance-based approach for 
    Type B and C testing. Additionally, the wording in the TSs would be 
    modified for the previous adoption of Option B on Type A testing and a 
    section added on the primary
    
    [[Page 14495]]
    
    containment leakage rate testing program.
        Date of issuance: February 27, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos: 207 and 188.
        Facility Operating License Nos. DPR-70 and DPR-75: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 14, 1998 (63 FR 
    2281).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated February 27, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: December 17, 1997.
        Brief description of amendments: The amendments extended the 
    surveillance interval of the containment spray nozzle air flow test to 
    ten years from five years.
        Date of issuance: March 11, 1998.
        Effective date: March 11, 1998.
        Amendment Nos.: Unit 1--Amendment No. 94; Unit 2--Amendment No. 81.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4325).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 11, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J.M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, OES Nuclear, Inc., 
    Pennsylvania Power Company, Toledo Edison Company, Docket No. 50-440 
    Perry Nuclear Power Plant, Unit 1, Lake County, Ohio.
    
        Date of application for amendment: December 23, 1997.
        Brief description of amendment: This amendment revised Technical 
    Specification 3.8.1, ``A.C. Sources--Operating,'' consistent with the 
    recommendations in NRC Generic Letter 94-01, ``Removal of Accelerated 
    Testing and Special Reporting Requirements for Emergency Diesel 
    Generators.''
        Date of issuance: March 12, 1998.
        Effective date: March 12, 1998.
        Amendment No.: 92.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4326).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 12, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: July 11, 1997, as supplemented 
    November 21, December 22, 1997, and February 6, 1998.
        Brief description of amendment: The amendment revised Technical 
    Specifications 3.7/4.7 and their associated Bases to incorporate Option 
    B of Appendix J to 10 CFR 50, and editorial changes to TS Table 4.7.2
        Date of Issuance: February 26, 1998.
        Effective date: February 26, 1998, with full implementation within 
    30 days.
        Amendment No.: 152.
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: (62 FR 45465). The 
    November 21, December 22, 1997, and February 6, 1998, letters did not 
    change the initial proposed no significant hazards determination.
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated February 26, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: November 20, 1997.
        Brief description of amendment: The amendment revised Technical 
    Specification (TS) 3.10 and its associated Bases to eliminate the use 
    of battery charger AB for meeting the requirement of the TS.
        Date of issuance: March 5, 1998.
        Effective Date: This license amendment is effective as of its date 
    of issuance, to be implemented within 30 days.
        Amendment No.: 153
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 31, 1997 (62 
    FR 68319).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 5, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: August 22, 1997, as supplemented 
    by letter dated September 18 and October 31, 1997.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to address the new low pressure CO2 suppression system 
    for the East and West Switchgear Rooms and more clearly describes the 
    separation of the two rooms.
        Date of Issuance: March 6, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 154.
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 8, 1997 (62 FR 
    52590). Information provided by letter dated October 31, 1997, did not 
    affect the original no significant hazards consideration.
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated March 6, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following
    
    [[Page 14496]]
    
    amendments. The Commission has determined for each of these amendments 
    that the application for the amendment complies with the standards and 
    requirements of the Atomic Energy Act of 1954, as amended (the Act), 
    and the Commission's rules and regulations. The Commission has made 
    appropriate findings as required by the Act and the Commission's rules 
    and regulations in 10 CFR Chapter I, which are set forth in the license 
    amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By April 24, 1998, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these
    
    [[Page 14497]]
    
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: February 5, 1998, as 
    supplemented February 12, March 3 and 5, 1998.
        Brief description of amendments: The amendments revised the 
    surveillance requirements in Technical Specification (TS) 4.6.1.2 
    (Requirement a). The change to the referenced TS adds a footnote 
    stating that the requirement for Type A testing will not apply to 
    certain instrument line penetrations.
        Date of issuance: March 10, 1998.
        Effective date: Both units, as of the date of issuance.
        Amendment Nos.: 173 and 146.
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: No. On February 5, 1998, the staff issued a Notice of 
    Enforcement Discretion, which was immediately effective and remained in 
    effect until this amendment was issued.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances, consultation with the State of Pennsylvania, 
    and final no significant hazards consideration determination are 
    contained in a Safety Evaluation dated March 10, 1998.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
        Dated at Rockville, Maryland, this 18th day of March 1998.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 98-7652 Filed 3-24-98; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
3/4/1998
Published:
03/25/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-7652
Dates:
March 4, 1998.
Pages:
14482-14497 (16 pages)
PDF File:
98-7652.pdf