96-7259. Biweekly Notice  

  • [Federal Register Volume 61, Number 60 (Wednesday, March 27, 1996)]
    [Notices]
    [Pages 13521-13540]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-7259]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 4, 1996, through March 15, 1996. The 
    last biweekly notice was published on March 13, 1996.
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By April 26, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing
    
    [[Page 13522]]
    Board will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: February 1, 1996
        Description of amendments request: The proposed amendment would (1) 
    revise Technical Specifications (TS) Sections 3/4.1.1.1, 6.9.1.9, and 
    6.9.1.10 to relocate the shutdown margin (reactor trip breakers open) 
    to the Core Operating Limits Report (COLR); (2) revise TS 3/4.3.2 
    (Tables 3.3-3 and 3.3-4), to specify an additional restriction for the 
    allowed low pressurizer pressure trip setpoint when reducing reactor 
    coolant system (RCS) pressure in Mode 3; (3) revise TS Section 2.2.1 
    (Table 2.2-1) to make it consistent with the footnote in TS Tables 3.3-
    3 and 3.3-4; and (4) revise TS Sections 3/4.5.2 and 3/4.5.3 to specify 
    an additional restriction to require that two emergency core cooling 
    system (ECCS) subsystems be operable in Mode 3 whenever the RCS cold 
    leg temperature is equal to or above 485 degrees F. In addition, the 
    Table of Contents and the Bases would be revised to be consistent with 
    these changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes do not significantly increase the 
    probability or consequences of an accident previously evaluated in 
    the Updated Final Safety Analysis Report (UFSAR). The proposed 
    changes to TS Tables 2.2-1, 3.3-3, and 3.3-4 to add additional 
    restrictions to the pressurizer pressure - low trip setpoint 
    requirements are more conservative than the current Technical 
    Specifications and will reflect the updated Mode 3 steam line break 
    safety analyses assumptions. The proposed changes to TS sections 3/
    4.5.2 and 3/4.5.3 to add additional restrictions to the requirement 
    to have two ECCS Subsystems operable are also more conservative than 
    the current Technical Specifications and will reflect the updated 
    Mode 3 steam line break safety analyses assumptions. Since these 
    changes are more restrictive, they would not contribute to the 
    initiation of any accident, nor would they increase the consequences 
    of an accident, but
    
    [[Page 13523]]
    they would enhance the plant response to a steam line break in Mode 
    3 to reduce consequences. The proposed changes to relocate the 
    shutdown margin - reactor trip breakers open to the COLR will have 
    no effect on the initiation or consequences of an accident. The 
    shutdown margin-reactor trip breakers open, which would be 
    determined using NRC approved analytical methods, as required by the 
    proposed changes, would ensure that the probability and consequences 
    of an accident would not increase. The changes to the titles of TS 
    3/4.5.2 and 3/4.5.3, and to the Table of Contents, are editorial and 
    have no effect on the operation of the plant or on any structures, 
    systems or components.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes do not create the possibility of an 
    accident of a new or different kind. The proposed changes to TS 
    Tables 2.2-1, 3.3-3, and 3.3-4, and TS section 3/4.5.2 and 3/4.5.3, 
    to add additional restrictions to the pressurizer pressure - low 
    trip setpoint requirement and add additional restrictions to the 
    requirement to have two ECCS Subsystems operable are more 
    conservative than the current Technical Specifications and will 
    reflect the updated Mode 3 steam line break safety analyses 
    assumptions. Since these changes are more restrictive, and therefore 
    bounded by the current TS, they would not contribute to the 
    initiation of any kind of new or different accident. The proposed 
    changes to relocate the shutdown margin -reactor trip breakers open 
    to the COLR will have no effect on the possibility of a new or 
    different kind of accident. The shutdown margin-reactor trip 
    breakers open, which would be determined using NRC approved 
    analytical methods as required by the proposed changes, would ensure 
    that there would be no possibility of a new or different kind of 
    accident from any accident previously evaluated. The changes to the 
    titles of TS 3/4.5.2 and 3/4.5.3, and to the Table of Contents, are 
    editorial and have no effect on the operation of the plant or on any 
    structures, systems or components.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed TS changes do not involve a reduction in any margin 
    of safety. The proposed changes to TS Tables 2.2-1, 3.3-3, and 3.3-
    4, and TS section 3/4.5.2 and 3/4.5.3, to add additional 
    restrictions to the pressurizer pressure - low trip setpoint 
    requirement and add additional restrictions to the requirement to 
    have two ECCS Subsystems operable are more conservative than the 
    current Technical Specifications and will reflect the updated Mode 3 
    steam line break safety analyses assumptions. Since these changes 
    are more restrictive, they do not involve a reduction in any margin 
    of safety as currently established by the existing TS. The proposed 
    changes to relocate the shutdown margin - reactor trip breakers open 
    to the COLR will have no effect on any margin of safety. The 
    shutdown margin - reactor trip breakers open would be determined 
    using NRC approved analytical methods as required by the proposed 
    changes, thus ensuring that there would be no reduction in any 
    margin of safety. The changes to the titles of TS 3/4.5.2 and 3/
    4.5.3, and to the Table of Contents, are editorial and have no 
    effect on the operation of the plant or on any structures, systems 
    or components.
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: February 15, 1996
        Description of amendment request: The proposed amendments would 
    revise Technical Specification (TS) 3.7 to add operability requirements 
    for the Keowee Hydro units during periods of commercial power 
    generation. These requirements are based on lake level and power level 
    of the Keowee Hydro units. Also, two surveillance requirements would be 
    added to TS 4.6 to (1) address periodic testing of the circuitry that 
    was added by the modification approved in NRC's SER dated August 15, 
    1995, and (2) add a load rejection surveillance to ensure that the 
    response of the Keowee Hydro units is bounded by the design criteria 
    used to develop the Keowee operating restrictions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) [Does not] involve a significant increase in the probability 
    or consequences of an accident previously evaluated:
        Each accident analysis addressed within the Oconee Final Safety 
    Analysis Report (FSAR) has been examined with respect to the change 
    proposed within this amendment request. The probability of any 
    Design Basis Accident (DBA) is not significantly increased by this 
    change. In addition, the consequences of the accidents are within 
    the bounds of the FSAR analyses.
        The design basis of the auxiliary electrical systems is to 
    supply the required engineered safeguards (ES) loads of one unit and 
    the safe shutdown loads of the other two units. The systems are 
    arranged so that no single failure will jeopardize plant safety. The 
    addition of the operability requirement and surveillances for the 
    Keowee Hydro units will ensure that the electrical systems can meet 
    their design basis.
        (2) [Does not] create the possibility of a new or different kind 
    of accident from any kind of accident previously evaluated:
        Addition of the operability requirement and surveillances will 
    not create a new or different kind of accident. The addition of the 
    circuitry which is covered by the operability requirement and 
    surveillances has been reviewed and approved by the NRC. Therefore, 
    operation of ONS [Oconee Nuclear Station] in accordance with this 
    Technical Specification amendment will not create any failure modes 
    not bounded by previously evaluated accidents. Consequently, this 
    change will not create the possibility of a new or different kind of 
    accident from any kind of accident previously evaluated.
        (3) [Does not] involve a significant reduction in a margin of 
    safety:
        The design basis of auxiliary electrical systems is to supply 
    the required ES loads of one Unit and safe shutdown loads of the 
    other two units. The ability of the Keowee Hydro units to provide 
    emergency power following an accident during a period of Keowee 
    Hydro commercial power generation was reviewed and approved by the 
    NRC in [an] SER dated August 15, 1995. Therefore, there will be no 
    significant reduction in any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: February 20, 1996
        Description of amendment request: The proposed amendments would 
    revise Technical Specifications (TS) 3.1.5, 3.1.10, and 4.1. The TS 
    changes would: (1) reduce the frequency for the concentrated boric acid 
    storage tank boron concentration surveillance, (2) delete the chemical 
    and radiochemical surveillance requirements for the reactor
    
    [[Page 13524]]
    coolant for Sr189 and Sr190, gross beta 
    activity, gross alpha activity, dissolved gas concentration in the 
    reactor coolant, and gross beta activity in the steam generator 
    feedwater, and (3) relocate the surveillance requirements for tritium, 
    chloride, fluoride and oxygen to the Selected Licensee Commitments 
    (SLC) Manual. The proposed changes would also delete some temperature 
    and pressure requirements on control rod operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The licensee has determined that operation of the 
    facility in accordance with the proposed amendments would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated:
        Each accident analysis addressed within the Oconee Final Safety 
    Analysis Report (FSAR) has been examined with respect to the 
    proposed amendment request. The probability of any Design Basis 
    Accident (DBA) is not significantly increased by the proposed 
    amendment due to the fact that the identified cause in the FSAR 
    accidents is not impacted. In addition, the consequences of the 
    accidents are within the bounds of the FSAR analyses since the 
    proposed amendment does not change the accident analysis methods or 
    assumptions described in the FSAR.
        (2) Create the possibility of a new or different kind of 
    accident from any kind of accident previously evaluated:
        The proposed amendment revises and eliminates several of the RCS 
    [Reactor Coolant System] chemistry Technical Specification 
    surveillance requirements. The changes in the surveillance 
    requirements do not alter the plant safety features or the method of 
    operation at ONS [Oconee Nuclear Station]. Therefore, operation of 
    ONS in accordance with the proposed Technical Specification will not 
    create any failure modes not bounded by previously evaluated 
    accidents.
        (3) Involve a significant reduction in a margin of safety.
        The proposed amendment does not impact the mitigation of any of 
    the accidents analyzed in the FSAR. Therefore, there is not a 
    significant reduction in the margin of safety associated with the 
    proposed amendment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: February 22, 1996
        Description of amendment request: The licensee has proposed to 
    increase the safety function lift setpoint tolerances for the safety 
    and relief valves that are listed in Surveillance Requirement 3.4.4.1 
    (Page 3.4-10) of the Technical Specifications TSs) for the Grand Gulf 
    Nuclear Station, Unit 1. The tolerances would be increased from the 
    current plus/minus 1 percent of the safety function (i.e., safety 
    relief valve) lift setpoint to plus/minus 3 percent.
        The frequency of verifying these setpoints would not be changed by 
    this amendment request. Also, the other surveillance requirements in 
    the TSs on these valves and the number of these valves required to be 
    operable are not being changed by this amendment request.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (NSHC) in Attachment 2 to its application of February 22, 
    1996.
        In its application, the licensee stated that it has used the NRC 
    staff's safety evaluation report (SER), NEDC 31753-P-A, issued in the 
    NRC letter of March 8, 1993, which evaluated General Electric (GE) 
    topical report NEDC-31753P, ``BWROG [BWR Owners' Group] In-Service 
    Pressure Relief Technical Specification Revision Licensing Topical 
    Report,'' dated February 1990.
        The licensee's NSHC analysis is presented below:
        Entergy Operations, Inc. is proposing that the Operating License 
    for Grand Gulf Nuclear Station (GGNS) be amended to increase the 
    tolerance of the safety function lift setpoints [from plus/minus 1%] 
    to plus/minus 3%. The GGNS Inservice Testing (IST) program controls 
    the frequency of safety relief valve (S/RV) testing as required by 
    the GGNS Operating License; therefore, this proposal will also 
    incorporate changes [concerning the setpoint tolerances] to 
    applicable IST procedures. GGNS will incorporate the recommendations 
    of the NEDC-31753-P-A [NRC staff's] SER, by resetting the safety 
    function [S/RV] lift setpoints for all tested valves to within plus/
    minus 1% of the design lift setpoint and increasing the test sample 
    size by two valves for each valve found outside the plus/minus 3% 
    safety function lift setpoint. S/RV test sample population will be 
    determined based upon the currently licensed ASME [American Society 
    of Mechanical Engineers] Boiler and Pressure Vessel Code.
        The commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 
    10CFR50.92(c). A proposed amendment to an operating license involves 
    no significant hazards if the operation of the facility in 
    accordance with the proposed amendment would not: (1) involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated; or (3) involve a significant reduction in a margin of 
    safety.
        Entergy Operations, Inc. has evaluated the no significant 
    hazards considerations in its request for a license amendment. In 
    accordance with 10CFR50.91(a), Entergy Operations, Inc. is providing 
    the following analysis of the proposed amendment against the three 
    standards in 10CFR50.92(c):
        a. No significant increase in the probability or consequences of 
    an accident previously evaluated results from this change.
        The GGNS safety design bases for the S/RVs are:
        ) Prevent overpressurization of the nuclear system that could 
    lead to failure of the reactor coolant pressure boundary,
        ) Provide automatic depressurization for small breaks in the 
    nuclear system,
        ) Permit verification of operability,
        ) Withstand adverse combinations of loadings and forces during 
    abnormal, accident, or special event conditions.
        The most limiting vessel overpressurization event is a closure 
    of all main steam isolation valves with a high flux scram. This 
    event was analyzed for GGNS using the minimum number of S/RVs 
    required by the GGNS Operating License. The safety function lift 
    setpoint tolerance used in the analysis bounds the proposed plus/
    minus 3% setpoint tolerance. The analysis indicates that the S/RVs 
    are capable of maintaining adequate margin below the Operating 
    License Reactor Coolant System Pressure of 1325 psig.
        Anticipated operational transients can also challenge the 
    operation of the S/RVs, for instance, Generator Load Reject without 
    Bypass. Analyses have been performed on the limiting events that 
    bound other pressure transient events using safety function limit 
    setpoint tolerances that bound the proposed plus/minus 3% tolerance 
    request. Fuel operating limits are based on the results of these 
    analyses; therefore, adequate fuel thermal margin is maintained.
        Plant transients and events that require the use of automatic 
    depressurization and the low-low set feature utilize the relief mode 
    of S/RV operation. This proposed change does not affect the relief 
    mode of S/RV operation.
        The verification of valve operability will still be performed in 
    accordance with the GGNS Inservice Testing Program, and S/RV safety 
    mode operability will be verified prior to reinstallation. Analysis 
    of the loads placed on each S/RV sub-system (discharge piping, 
    spargers and associated components) verifies that adequate margin 
    exists to ensure that the
    
    [[Page 13525]]
    overpressurization system can perform its designed function.
        The negative tolerance of the safety function lift setpoint 
    remains above the highest setpoint of the S/RV relief mode, and 
    therefore normal vessel pressure. This margin provides reasonable 
    assurance that inadvertent opening of an S/RV will not occur during 
    power operations.
        GGNS will replace each S/RV removed for IST program testing with 
    an S/RV that has been reset to within plus/minus 1% of the designed 
    safety function lift setpoint. During each refueling outage, at 
    least six of the installed S/RVs will be tested for safety lift 
    setpoint in accordance with the current IST program plant 
    procedures. This sample population is in agreement with the current 
    ASME Boiler and Pressure Vessel Code requirements for the GGNS IST 
    program, and is more restrictive than the ANSI/ASME OM-1-1981 
    requirement upon which the setpoint tolerance was based. For S/RV 
    setpoint testing ([the] as-found [setpoint]), additional valves will 
    be tested if the as-found setpoint is outside plus/minus 3% of its 
    designed safety function lift setpoint. Sample expansion will be 
    consistent with the NEDC 31753-P-A SER requirement of two additional 
    valves per valve failure.
        The GGNS UFSAR currently requires at least fifty percent of the 
    installed valves to be removed and tested during each refueling 
    outage. GGNS FSAR Questions & Responses  211.49 discusses 
    the bases for this requirement. The concern regarded the performance 
    of S/RVs installed in operating plants at the time of GGNS 
    construction and licensing, and that new plants should have 
    significantly better performing S/RVs. The fifty percent requirement 
    provides a very conservative margin of testing to demonstrate that 
    no common cause of S/RV failure occurs within any one operating 
    cycle. The minimum testing of six valves proposed for each outage, 
    with additional testing for each failure from the initial test 
    population, provides reasonable assurance that no common cause 
    failure is occurring without early detection. [The minimum testing 
    of six valves is in agreement with the current ASME Code 
    requirements and is consistent with the current industry practices 
    that was accepted in the NRC staff's safety evaluation report, NEDC 
    31753-P-A.]
        One of the major factors in the requirement of additional 
    testing population beyond ASME Boiler and Pressure Vessel Code is 
    many of the older plants were experiencing failures with multiple 
    stage pilot operated S/RVs. The safety function of this type of S/RV 
    requires operation of a pilot valve that is susceptible to excessive 
    leakage and corrosive bonding to cylinder walls; thereby preventing 
    proper safety function operation. The GGNS Dikkers S/RVs are direct 
    acting, and do not require the operation of a pilot valve for the 
    safety function. The Dikkers S/RV Instruction Manual recommends ``to 
    replace part of the installed valves each maintenance stop 
    (refueling outage)'', and does not prescribe any particular [number 
    of valves to be tested].
        Therefore, no significant increase in the probability or 
    consequences of an accident previously evaluated results from this 
    proposed change.
        b. This change would not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        The plant specific analyses verify that each S/RV will still 
    perform the intended function of preventing overpressurization of 
    the nuclear system. The vessel will have adequate margin below the 
    Operating License Reactor Coolant System Pressure of 1325 psig, and 
    plant system response will not deviate from the expected sequence of 
    events. Each system, structure, and component that communicates with 
    the reactor vessel has been verified to be within its design and 
    operational margin, and no unanticipated plant transients will occur 
    as a result of the safety lift function setpoint tolerance change.
        The negative tolerance of the safety function lift setpoint 
    remains above the highest setpoint of the S/RV relief mode, and 
    therefore normal vessel pressure. This margin provides reasonable 
    assurance that inadvertent opening of an S/RV will not occur during 
    power operations.
        This proposed change does not add any new systems, structures or 
    supports, nor does it introduce new S/RV operating modes.
        Therefore, this change would not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        c. This change would not involve a significant reduction in the 
    margin of safety.
        The increase in the S/RV safety function lift tolerance has been 
    analyzed for bounding limiting events and accident conditions. [The 
    safety function lift setpoint tolerance used in the analysis bounds 
    the proposed plus/minus 3% setpoint tolerance.] No condition exists 
    that reduces the margin of safety on the reactor coolant pressure 
    boundary or any system, structure or component that is required to 
    operate during vessel overpressurization events. Fuel operating 
    limits are based on the results of these analyses; therefore, 
    adequate fuel thermal margin is maintained.
        [The negative tolerance of the safety function lift setpoint 
    remains above the highest setpoint of the S/RV relief mode, and 
    therefore normal vessel pressure. This margin provides reasonable 
    assurance that inadvertent opening of an S/RV will not occur during 
    power operations.]
        Therefore, this change would not involve a significant reduction 
    in the margin of safety.
        Based on the above evaluation, Entergy Operations, Inc. has 
    concluded that operation in accordance with the proposed amendment 
    involves no significant hazards considerations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: February 22, 1996
        Description of amendment request: The amendment proposes to delete 
    a specification which requires a thorough inspection of the Emergency 
    Diesel Generator (EDG) every 24 months during shutdown. In addition 
    this Technical Specification proposes to delete the phrase ``in any 
    thirty day period'' from a specification concerning Allowed Outage time 
    (AOT).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        GPU Nuclear has determined that this [technical specification 
    change request] TSCR poses no significant hazard as defined by the 
    NRC in 10 CFR 50.92.
        1. State the basis for the determination that the proposed 
    activity will or will not increase the probability of occurrence of 
    the consequences of an accident.
        The proposed activity deletes the requirement to inspect EDGs 
    during shut down from the Technical Specifications. It further 
    modifies the operability of a single EDG for a limited and defined 
    period of time. These changes do not affect the design or 
    performance of the EDGs or their ability to perform their design 
    function. Analysis using PRA techniques indicates the changes do not 
    significantly increase the probability or consequences of an 
    accident.
        2. State the basis for the determination that the activity does 
    or does not create a possibility of an accident or malfunction of a 
    different type than any previously identified in the SAR.
        The EDGs are not the source of any accident described in the 
    SAR. These changes do not modify the design or performance of the 
    EDGs and do not affect plant functions or actions. Therefore, the 
    proposed change does not create the possibility of an accident or 
    malfunction of a different type than those previously identified.
        3. State the basis for the determination that the margin of 
    safety is not reduced. The proposed changes are designed to improve 
    EDG reliability and availability during shutdown periods by 
    providing flexibility in the scheduling and performance of 
    maintenance. The surveillance intervals are unchanged and 
    operability requirements are only modified to an acceptable degree. 
    The proposed activity does not alter the basis of
    
    [[Page 13526]]
    any technical specification that is related to the establishment or 
    maintenance of a nuclear safety margin. Therefore, the margin of 
    safety is not significantly reduced by this action.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: February 23, 1996
        Description of amendment request: The proposed change to the 
    Technical Specifications would allow the implementation of 10 CFR 50, 
    Appendix J, Option B.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        GPU Nuclear has determined that this TSCR [technical 
    specification change request] involves no significant hazards 
    considerations as defined by NRC in 10 CFR 50.92.
        The major changes from the existing Oyster Creek Technical 
    Specifications requested in accordance with the Option B 
    requirements:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident or 
    malfunction of equipment important to safety as previously evaluated 
    in the Safety Analysis Report.
        The proposed change implements Option B of 10 CFR 50, Appendix J 
    on performance based containment leakage testing. The proposed 
    change does not involve a change to the plant design or operation. 
    Therefore, the proposed change does not affect any of the parameters 
    or conditions that contribute to initiation of any of the analyzed 
    accidents or malfunctions. The proposed change does request an 
    allowable extension of containment testing. Therefore, a 
    hypothetical leak could remain undetected for a greater period of 
    time. This slight increase in risk has been determined to be 
    insignificant as:
        Type A Testing
        NUREG 1493 determined that the effect of containment leakage on 
    overall accident risk is small as risk is dominated by accident 
    sequences that result in the failure or bypass of the containment. 
    Industry wide PCILRTs have demonstrated that only a small fraction 
    of the leaks discovered during testing exceeded acceptance criteria, 
    and that the leak rate has been only marginally above the acceptable 
    limit. Only 3% of all leaks can be detected only by PCILRT, 
    therefore, only 3% of the theoretical leaks are affected by the 
    extension to the Type A test interval. Experience at Oyster Creek 
    agrees with the industry wide data in that the majority of the 
    detected leakage from the primary containment is found through Type 
    B and C testing.
        NUREG 1493 found that these observations, together with the 
    insensitivity of reactor accident risk to the containment leakage 
    rate, demonstrates that increasing the Type A leakage test intervals 
    would have a minimal impact on public risk.
        Type B and C Testing
        Penetrations are designed to ensure reliability of the 
    containment isolation function. Type B penetrations use a double 
    passive seal (e.g. o-ring, gasket) and Type C penetrations use a 
    double isolation valve design to ensure reliability of the isolation 
    function. Because valves perform the isolation function actively, 
    they are more likely to fail on demand (e.g. failure to completely 
    close on demand). To address this failure mode, Type C valves are 
    subjected to increased design constraints and testing to ensure both 
    acceptable leak rates and stroke times. The proposed change does not 
    alter the installation, operation, operating environment, or testing 
    method of these valves. Therefore, the proposed change does not 
    introduce any new component failure modes, nor does it affect the 
    probability of occurrence of any existing evaluated failure mode.
        The failure of any single penetration barrier (isolation valve 
    or passive seal) does not cause penetration failure. Therefore, a 
    double failure would have to occur to cause a failure of the 
    penetration and affect containment. Additionally, the proposed 
    change does not change the acceptance criteria for acceptable 
    leakage testing.
        The proposed change does not alter plant design or operation, 
    nor does it alter the allowable maximum leakage rate limit. Thus, 
    the proposed change does not affect the probability of occurrence 
    nor the consequences of any evaluated accident or malfunction of 
    equipment important to safety.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of an accident or 
    malfunction different from any accident or malfunction previously 
    evaluated.
        The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that could contribute to 
    initiation of any accidents. This change only involves the reduction 
    in Type A, B and C test frequencies, and the Type A test pressure.
        Type A Testing
        The only changes proposed to the Type A testing are to frequency 
    and test pressure. As the proposed test pressure is grater than the 
    existing test pressure, no new type of accident or malfunction is 
    created, and the increase in pressure provides an additional margin 
    of safety. The increase in pressure provides an additional margin of 
    safety. The increase in surveillance interval cannot introduce any 
    new type of accident or malfunction.
        The PCILRT is presently performed at 20 psig. Performance of the 
    PCILRT at Pa (35 PSIG) will provide a more direct leak rate for 
    analysis.Pa is the design pressure of the torus (the drywell 
    design pressure is 44 psig, but the torus is non isolable form the 
    drywell. Therefore, Pa will not create the possibility of the 
    failure of the torus due to overpressurization. No new accident 
    modes can be created by extending the test intervals. No safety 
    related functions or components are altered as a result of this 
    change. Therefore, no new accident or malfunction different form 
    those evaluated in the Safety Analysis Report can result due to the 
    increase in test pressure or increase in surveillance interval.
        Type B and C Testing
        The proposed change only deals with the frequency of performing 
    Type B and C testing. It does not change what components are tested 
    or the method of testing. There is no proposed change to the design 
    or operation of the plant. Therefore, no new accident or malfunction 
    different form those evaluated in the Safety Analysis Report can 
    result due to the increase in test pressure or increase in 
    surveillance interval.
        3. Operation of the facility in accordance with the proposed 
    amendment would not decrease the margin of safety as defined in the 
    bases of the Technical Specifications.
        Type A Testing
        Except for the method of defining the test frequency and 
    pressure at which the PCILRT is performed, the methods for 
    performing the actual test are not changed. However, the proposed 
    change can increase the probability that an increase in leakage 
    could go undetected for an extended period of time. NUREG 1493 has 
    determined that under several different accident scenarios, the 
    increased risk of radioactivity release from containment is 
    negligible with the implementation of these proposed changes.
        Type B and C Testing
        The proposed change only affects the frequency of Type B and C 
    testing. The methods for performing the actual test are not changed. 
    The design or operation of Type B and C components are not changed. 
    The proposed change will result in a longer interval between tests 
    of good performing Type B and C components.
        The margin of safety that has the potential of being impacted by 
    the proposed change involves the offsite dose consequences of 
    postulated accidents which are directly related to containment 
    leakage rate. The containment isolation system is designed to limit 
    leakage to La, which is defined by the Oyster Creek Technical 
    Specifications to be 1.0 percent by weight of the containment air at 
    35 psig per 24 hours. The limitation on
    
    [[Page 13527]]
    containment leakage rate is designed to ensure the total leakage 
    volume will not exceed the value assumed in the accident analyses at 
    the peak accident pressure (Pa). The margin of safety for the 
    offsite dose consequences of postulated accidents directly related 
    to the containment leakage rate is maintained by meeting the 1.0 
    La acceptance criteria. The La value is not being modified 
    by this proposed Technical Specification change request.
        Therefore, the margin of safety as defined in the bases for the 
    Technical Specification will not be reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of amendment requests: February 22, 1996 (AEP:NRC:0659AA)
        Description of amendment requests: The proposed amendments would 
    revise the technical specifications to remove the requirement that the 
    Operations Superintendent must hold or have held a Senior Operator 
    License at Cook Nuclear Plant, or a similar reactor. In addition, a 
    mid-level operations manager will only be required to hold a Senior 
    Operator License if the Operations Superintendent does not hold one.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Per 10 CFR 50.92, this proposed change does not involve a 
    significant hazards consideration because the change does not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated,
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. involve a significant reduction in a margin of safety.
        Criterion 1
        The amendment request does not involve a significant increase in 
    the probability or consequences of [an] accident previously 
    evaluated because the proposed change to the Technical Specification 
    does not affect the assumptions, parameters, or results of any UFSAR 
    [updated final safety analysis report] accident analysis. The 
    proposed amendment does not modify any existing equipment. It is 
    concluded that the changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Criterion 2
        The proposed change does not involve physical changes to the 
    plant or changes in plant operating configuration. The proposed 
    change updates the requirements for the Operations Superintendent. 
    Thus, it is concluded that the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Criterion 3
        The proposed change updates the requirements for Operations 
    Superintendent. There is no reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Indiana Michigan Power Company, Docket No. 50-316, Donald C. Cook 
    Nuclear Plant, Unit No. 2, Berrien County, Michigan
    
        Date of amendment request: March 12, 1996 (AEP:NRC:1248)
        Description of amendment request: The proposed amendment would 
    remove the technical specifications related to shutdown and control rod 
    position indication while in modes 3, 4, and 5. The change would make 
    the Unit 2 technical specifications consistent with the Unit 1 
    technical specifications and the Standard Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Per 10 CFR 50.92, this proposed change does not involve a 
    significant hazards consideration because the change does not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated,
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. involve a significant reduction in a margin of safety.
        Criterion 1
        The boron concentration in the reactor coolant system will be 
    high enough to assure adequate SDM in modes 3, 4, and 5. The 
    calculation to obtain the required boron concentration takes into 
    account the position of the rods. Shutdown margin is assumed as an 
    initial condition in the safety analysis. The safety analysis 
    establishes a SDM that ensures specified acceptable fuel design 
    limits are not exceeded. As long as the SDM is satisfied, no change 
    in the probability or consequences of an accident previously 
    evaluated will result from the proposed deletion of the ``position 
    indicator - shutdown'' specification. It is noted that this change 
    is consistent with the new ISTS approved by the NRC as NUREG-1431, 
    Rev. 1.
        Criterion 2
        The ability to insert the control and shutdown rods provided by 
    the rod control system is not affected by the OPERABILITY status of 
    the ARPI system. As mentioned previously, the reactor coolant system 
    boron concentration will be high enough to assure adequate SDM is 
    maintained. Therefore, it is concluded that the proposed changes do 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        Criterion 3
        The margin of safety requirements are not affected by the 
    removal of this T/S. The required SDM which is an initial condition 
    in the safety analysis, is unaffected since the reactor coolant 
    system boron concentration is increased to address the potential 
    ``all rods out'' configuration. Based on these considerations, it is 
    concluded that the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of amendment request: November 29, 1995
        Description of amendment request: The proposed amendment would
    
    [[Page 13528]]
    modify the Technical Specifications to remove the requirement for 
    additional pressure relief by a residual heat removal (RHR) spring 
    relief valve during low temperature overpressure protection (LTOP) 
    conditions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change to delete Technical Specification 3.4.D.3b 
    has been evaluated against the standards of 10 CFR 50.92 and has 
    been determined not to involve a significant hazards consideration. 
    This proposed change does not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously analyzed. The Power Operative 
    Relief Valves (PORVs) remain operable to mitigate any LTOP event. 
    Thus, this change does not result in an increase in the probability 
    or consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated. Removing the RHR spring relief valve as 
    an additional relief requirement does not create the possibility of a 
    new or different kind of accident since the proposal involves neither a 
    hardware modification nor the creation of a unique operating condition.
        3. Involve a significant reduction in a margin of safety. 
    Removing the RHR spring relief valve as an additional requirement 
    does not change the results of any of the FSAR Chapter 14 events. 
    The PORVs remain operable to maintain the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011NRC Deputy Director: 
    John Zwolinski
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of amendment request: November 29, 1995
        Description of amendment request: The proposed amendment would 
    modify Technical Specification (TS) 3.14 to decrease the maximum steam 
    generator (SG) primary-to-secondary leakage rate from 0.15 gpm to 0.10 
    gpm and would modify TS 4.10 by revising the requirements for 
    unscheduled SG tube inspections that are performed on each SG following 
    a primary-to-secondary tube leak.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    A steam generator leakage assumption greater than the proposed 0.10 
    gpm/SG limit has been used in the FSAR [Final Safety Analysis 
    Report] Chapter 14 safety analyses. Thus, the FSAR Chapter 14 safety 
    analyses remain bounding. Assuring that an adequate leakage limit 
    exists that initiates corrective actions in a timely manner is 
    important to ensuring a steam generator tube rupture event does not 
    take place. This change modifies the steam generator post-leakage 
    testing requirements to focus inspections on leaking tubes and areas 
    likely to produce similar leakage, in lieu of an expanded test 
    campaign of all three steam generators. Without this change, 
    Technical Specifications require inspection of 3% of the tubes in 
    each steam generator. By inspecting the critical areas of the 
    affected steam generator and possibly expanding inspections to the 
    critical areas of the remaining steam generators, the probability 
    and/or consequences of previously evaluated accidents (e.g., steam 
    generator tube rupture) are not increased.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The proposed changes will not involve a modification to 
    existing hardware at the plant. The decrease in the maximum 
    allowable steam generator primary leakage rate tends to provide 
    additional time for operator action to take place which, if timely 
    enough, would avoid the consequences of a tube rupture event. The 
    proposed inspection campaign requires inspection of the critical 
    area and may be expanded to the other steam generators to ensure 
    that additional tubes will not fail due to similar causes. This 
    modified inspection campaign does not introduce the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety. The FSAR Chapter 14 safety analyses assume a 
    higher steam generator leakage rate and therefore remain 
    conservative. The proposed reduction in the allowable leakage 
    provides a greater margin of safety since it is more conservative 
    than the present value. This change modifies inspection requirements 
    of Technical Specifications and does not impact the plant design or 
    equipment. The modified inspection requirements following a plant 
    shutdown due to tube leakage concentrate steam generator tube 
    inspections in those areas believed to be most susceptible to flaws. 
    For these reasons, we believe the proposed changes increase the 
    margin of safety by inspecting the critical areas of the steam 
    generator(s) in lieu of additional random inspections.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 329 Bath Road, Brunswick, ME 04011NRC Deputy Director: 
    John Zwolinski
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of amendment request: November 8, 1995
        Description of amendment request: The amendment request would 
    revise the Technical Specifications (TS) for the jet pumps to be 
    consistent with the limiting conditions for operation and surveillance 
    requirements in the Standard Technical Specifications for General 
    Electric Plants (NUREG-1433).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ...The proposed change does not involve an [significant hazards 
    consideration] SHC because the change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The new LCO [Limiting Condition for Operation] does not diminish 
    the existing requirement that all jet pumps must be operable, nor 
    does it affect the time available to achieve cold shutdown should a 
    pump become inoperable. The new LCO does eliminate the ability to 
    continue to operate with the indication (but not the function) of a 
    single jet pump inoperable. This does not increase the possibility 
    of an unnecessary plant shutdown due to inoperable instrumentation 
    since sufficient flexibility exists in the surveillance requirement 
    so that operability of the jet pumps can be verified. This change 
    eliminates the LCO that allowed continued operation with conditions 
    that could potentially mask an inoperable pump. The new LCO is more 
    limiting in ensuring that the plant is operated in a condition for 
    which accidents were analyzed.
        The new surveillance requirement provides a more accurate method 
    of ensuring
    
    [[Page 13529]]
    the jet pumps remain operable. The new surveillance criteria are 
    more sensitive to jet pump failures and the degradation of the jet 
    pumps prior to failure.
        Based on the above, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The new LCO and surveillance does not change the manner in which 
    the plant is operated, nor does it reduce the operability 
    requirements of any jet pump, Therefore, no new or different kind of 
    accident can be created by the new specification. The surveillances 
    that will be performed do not require any new hardware or plant 
    evolutions. Therefore, the proposed change to the LCO and 
    surveillance cannot create the possibility of a new or different 
    kind of accident.
        3. Involve a significant reduction in the margin of safety.
        The margin of safety that currently exists is not diminished by 
    this change. The requirement to place the reactor in cold shutdown 
    within 24 hours should a jet pump become inoperable is maintained. 
    The LCO which allowed continued operation with indication for one 
    pump inoperable has been eliminated.
        The new surveillance requirement continues to demonstrate the 
    operability of the jet pumps and during operation, continues to be 
    performed at the same interval as in the current technical 
    specifications. The note (which allows the surveillance to be 
    deferred until four hours after the associated recirculation loop is 
    in operation and 24 hours after exceeding 25% of rated thermal 
    power) does not significantly affect the margin of safety. The time 
    that the unit would be operating in these conditions would be small, 
    and the stress placed on the pump at less than 25% power is lower.
        Based on the above, this change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London, 
    Connecticut
    
        Date of amendment request: November 3, 1995
        Description of amendment request: The proposed amendment will 
    extend the allowed outage time from 48 hours to 7 days for an emergency 
    core cooling system train that is declared inoperable as a result of an 
    inoperable low pressure safety injection subsystem.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Pursuant to 10CFR50.92, Northeast Nuclear Energy Company (NNECO) 
    has reviewed the proposed change to extend the allowed outage time 
    (AOT) for an inoperable low pressure safety injection (LPSI) 
    subsystem from the existing limit of 48 hours to 7 days. In 
    addition, the change to modify the completion time for the Action 
    Statement and the criteria for the Surveillance Requirements were 
    also reviewed. NNECO concludes that these changes do not involve a 
    significant hazards consideration (SHC) since the proposed change 
    satisfies the criteria in 10CFR50.92(c). That is, the proposed 
    change does not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed amendments for Millstone Unit No. 2 will extend the 
    action completion AOT for a single inoperable LPSI train from 48 
    hours to 7 days. A LPSI subsystem is designed as a part of each 
    emergency core cooling system (ECCS) train to supplement safety 
    injection tank inventory during the early stages of mitigating a 
    design basis accident (DBA). As such, components of the LPSI 
    subsystem are not accident initiators, and an extended AOT to 
    restore operability of an inoperable LPSI subsystem would not 
    increase the probability of occurrence of accidents previously 
    analyzed.
        The safety analyses for Millstone Unit No. 2 demonstrates that 
    ECCS performance acceptance criteria are satisfied with only one of 
    the two redundant ECCS trains operating during the postulated DBA. 
    The proposed technical specification revisions involve the AOT for a 
    single inoperable LPSI subsystem, and do not change the conditions 
    assumed for the minimum amount of operating equipment needed for 
    accident mitigation. Therefore, the consequences of an accident 
    previously evaluated will not be significantly increased.
        In addition, CE NPSD-995 recognizes that when an ECCS train is 
    inoperable due to a LPSI subsystem being unavailable, due either to 
    being declared inoperable (by failing a surveillance requirement) or 
    is intentionally taken out-of-service (for corrective or preventive 
    maintenance), the core damage frequency (CDF) during power operation 
    increases. The results of the PRA presented in CE NPSD-995 show that 
    the proposed increase in the ECCS AOT (due to LPSI unavailability) 
    from 48 hours to 7 days does not cause a significant increase in the 
    overall CDF of Millstone Unit No. 2.
        The analyses indicate that continued plant operation with a 
    single LPSI subsystem out-of-service may result in a small increase 
    in ``at power risk;'' however, that risk increase will be negligibly 
    small and controlled effectively via the Maintenance Rule and the 
    risk monitor program that minimizes the outage time and prevents 
    entering into an unacceptable risk configuration. In addition, the 
    proposed AOT extension for the LPSI subsystem is evaluated as having 
    negligible impact on the large early radiological release 
    probability for Combustion Engineering pressurized water reactors in 
    the event of a design basis accident.
        Therefore, operation in accordance with the proposed amendment 
    would not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed amendment will not change the physical plant or the 
    modes of plant operation defined in the technical specifications. 
    The changes do not involve the addition or modification of equipment 
    nor do they alter the design of plant systems. Therefore, operation 
    of Millstone Unit No. 2 in accordance with its proposed amendment 
    would not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The margin of safety associated with the ECCS train is 
    established by acceptance criteria for system performance defined in 
    10CFR50.46. The proposed amendment will not change this acceptance 
    criteria nor the operability requirements for equipment that is used 
    to achieve such performance as demonstrated in the Millstone Unit 
    No. 2 safety analyses. Moreover, an integrated assessment of the 
    risk impact of extending the AOT for a single inoperable LPSI train 
    has concluded that the risk contribution is small. Therefore, 
    operation of Millstone Unit No. 2 in accordance with its proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
    
    [[Page 13530]]
    
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: September 12, 1995
        Description of amendment request: The amendment would revise and 
    reformat Technical Specification (TS) 6.3.1 to add the requirement that 
    the Assistant Operations Manager shall hold a senior reactor operator 
    (SRO) license if the Operations Manager does not hold an SRO license 
    for Millstone Unit 3. Also the footnote would be deleted from TS 6.3.1 
    that previously granted a one-time three year exception to the 
    qualification requirements for the Operations Manager and an exception 
    for the Assistant Operations Manager to hold a license instead of the 
    Operations Manager.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ...The proposed change does not involve an [significant hazards 
    consideration] SHC because the change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed change affects an administrative control, which was 
    based on the guidance of ANSI N18.1-1971. ANSI N18.1-1971 
    recommended that the Operations Manager hold an SRO license. The 
    current guidance in Section 4.2.2 of ANSI/ANS 3.1-1987 recommends, 
    as one option, that the Operations Manager have held a license for a 
    similar unit and the Operations Middle Manager hold an SRO license. 
    While the Operations Middle Manager position does not exist at 
    Millstone Unit No. 3, [Northeast Nuclear Energy Company] NNECO has 
    created the position of Assistant Operations Manager. The individual 
    in this position would meet the requirements for, and would have 
    responsibilities as recommended in, ANSI/ANS 3.1-1987 for the 
    Operations Middle Manager position.
        Therefore, the proposed change requests an exception to ANSI 
    N18.1-1971 to allow use of ANSI/ANS 3.1-1987 in a limited 
    circumstance. Specifically, the proposed revision to Technical 
    Specification 6.3.1 would require the Operations Manager to either 
    hold an SRO license at Millstone Unit No. 3 or have held an SRO at a 
    [pressurized water reactor] PWR.
        If the Operations Manager does not hold an SRO license at 
    Millstone Unit No. 3, the specification will require the Assistant 
    Operations Manager to hold, and continue to hold, an SRO license. 
    The proposed change includes the requirement for the Operations 
    Manager to have held a license for a similar unit (a PWR) in 
    accordance with Section 4.2.2 of ANSI/ANS 3.1-1987. For those areas 
    of knowledge that require an SRO license, the Assistant Operations 
    Manager will provide the technical guidance normally provided by the 
    Operations Manager.
        The proposed change does not alter the design of any system, 
    structure, or component, nor does it change the way plant systems 
    are operated. It does not reduce the knowledge, qualifications, or 
    skills of licensed operators, and does not affect the way the 
    Operations Department is managed by the Operations Manager. The 
    Operations Manager will continue to maintain the effective 
    performance of his personnel and ensure the plant is operated safely 
    and in accordance with the requirements of the operating license. 
    Additionally, the Control Room Operators will continue to be 
    supervised by the licensed Shift Supervisors.
        The proposed change does not detract from the Operations 
    Manager's ability to perform his primary responsibilities. In this 
    case, by having previously held an SRO license, the Operations 
    Manager has achieved the necessary training, skills, and experience 
    to fully understand the operation of plant equipment and the watch 
    requirements for operators. In summary, the proposed change does not 
    affect the ability of the Operations Manager to provide the plant 
    oversight required of his position. Thus, it does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed change to Technical Specification 6.3.1 does not 
    affect the design or function of any plant system, structure, or 
    component, nor does it change the way plant systems are operated. It 
    does not affect the performance of NRC licensed operators. Operation 
    of the plant in conformance with technical specifications and other 
    license requirements will continue to be supervised by personnel who 
    hold an NRC SRO license. The proposed change to Technical 
    Specification 6.3.1 ensures that the Operations Manager will be a 
    knowledgeable and qualified individual to have held an SRO license 
    at a PWR. Based on the above, the proposed change does not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The proposed change involves an administrative control that is 
    not related to the margin of safety. The proposed change does not 
    reduce the level of knowledge or experience required of an 
    individual who fills the Operations Manager position, nor does it 
    affect the conservative manner in which the plant is operated. The 
    Control Room Operators will continue to be supervised by personnel 
    who hold an SRO license. Thus, the proposed change does not involve 
    a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: November 21, 1995
        Description of amendment request: The licensee proposes to change 
    Technical Specification Section 1.33 and Bases Sections 3/4.3.3.9 and 
    3/4.3.3.10, and 3/4.11.2.1. The changes clarify the definition of 
    source check to include a source check from a light emitting diode 
    (LED), as well as from ionizing radiation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ... NNECO concludes that these changes do not involve a 
    significant hazards consideration since the proposed changes satisfy 
    the criteria in 10CFR50.92(c). That is, the proposed changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed changes to the definition of source check clarifies 
    the source check for the liquid and gaseous effluent radiation 
    monitors. These monitors do not provide a safety function and only 
    serve to provide radiological information to plant operators, 
    therefore, the changes will not increase the probability or 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes to the definition of source check have no 
    effect on the ability of the monitors to perform their designed 
    function. The clarification to the surveillance do not involve any 
    physical modifications to any equipment, structures, or components. 
    The monitors already have the internal LEDs which were originally 
    used to perform the source check. The proposed changes have no 
    impact on design basis accidents, and the changes will not modify 
    plant response or create a new or unanalyzed event.
        3. Involve a significant reduction in the margin of safety.
        
    [[Page 13531]]
    
        The proposed changes to the definition of source check do not 
    have any impact on the protective boundaries and, therefore, have no 
    impact on the safety limits for these boundaries. The 
    instrumentation associated with these changes do not provide a 
    safety function and only serve to provide radiological information 
    to plant operators. The instrumentation has no affect on the 
    operation of any safety-related equipment. As such, these changes 
    have no impact on the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    PECO Energy Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Dockets Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station, Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: February 15, 1996
        Description of amendment request: The amendment changes the 
    Technical Specifications to implement 10 CFR Part 50, Appendix J, 
    Option B, by creating Technical Specification Section 5.5.12, ``Primary 
    Containment Leakage Rate Testing Program,'' which refers to Regulatory 
    Guide 1.163, ``Performance-Based Containment Leakage-Test Program.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) The proposed changes do not involve a significant increase in 
    the probability or consequences of any accident previously 
    evaluated.
        The adoption of 10 CFR 50, Appendix J Option B will not involve 
    a significant increase in the probability or consequences of any 
    accident previously evaluated. The proposed changes to the TS 
    [Technical Specifications] reflect the use of the performance-based 
    containment leakage-testing program. The USNRC has approved the use 
    of a performance-based option for containment leakage testing 
    programs when it amended 10 CFR 50, Appendix J (60 FR 49495). For 
    adoption of the revised regulation, licensees are required to 
    incorporate into their TS, by general reference, the USNRC 
    regulatory guide or other plant-specific implementing document used 
    to develop their performance-based leakage testing program. A new 
    Administrative Control subsection (5.5.12, ``Primary Containment 
    Leakage Rate Testing Program'') has been added that requires the 
    establishment and maintenance of a Primary Containment Leakage Rate 
    Testing Program. The TS will still require the performance of a 
    periodic general visual inspection of the containment to ensure 
    early detection of any structural deterioration of the containment 
    that may occur.
        As concluded in NUREG-1493, given the insensitivity of risk to 
    containment leakage rate and the small fraction of leakage paths 
    detected solely by ILRT [Integrated Leak Rate Test] testing, 
    increasing the interval between ILRTs is possible with minimal 
    impact on public risk. Additionally, performance-based alternatives 
    to current LLRT [Local Leak Rate Test] requirements are feasible 
    without significant risk impacts. Additionally, these changes will 
    not alter any safety limits which ensure the integrity of fuel 
    barriers, and will not result in a significant increase to onsite or 
    offsite dose.
        No physical changes are being made to the plant, nor are there 
    any changes being made in the operation of the plant as a result of 
    these changes which could involve a significant increase in the 
    probability or consequences of any accident previously evaluated. 
    Additionally, these changes will not alter the operation of 
    equipment assumed to be available for the mitigation of accidents or 
    transients.
        2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The adoption of 10 CFR 50, Appendix J Option B will not create 
    the possibility of a new or different type of accident from any 
    previously evaluated. These changes to the PBAPS, Units 2 and 3 TS 
    will not involve any changes to plant systems, structures or 
    components (SCCs) which could act as new accident initiators. These 
    changes will not impact the manner in which SSCs are tested such 
    that a new or different type of accident from any previously 
    evaluated could be created.
        3) The proposed changes do not result in a significant reduction 
    in the margin of safety.
        No margins of safety are reduced as a result of the proposed 
    adoption of 10 CFR 50, Appendix J Option B. As stated previously, 
    the USNRC has approved the use of this performance-based option for 
    containment leakage testing programs when it amended 10 CFR 50, 
    Appendix J (60 FR 49495). These changes will not impact core limits 
    or any other parameters that are used in the mitigation of a UFSAR 
    [Updated Final Safety Analysis Report] design-basis accident or 
    transient. Additionally, these changes do not introduce any hardware 
    changes, and will not alter the intended operation of plant 
    structures, systems or components utilized in the mitigation of 
    UFSAR design-basis accidents or transients. These changes will not 
    introduce any new failure modes of plant equipment not previously 
    evaluated.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    Pennsylvania 19101
        NRC Project Director: John F. Stolz
    Pennsylvania Power and Light Company, Docket No. 50-387, 
    Susquehanna Steam Electric Station, Unit 1, Luzerne County, 
    Pennsylvania
        Date of amendment request: January 26, 1996
        Description of amendment request: The proposed amendment removes 
    three pressure relief valves from Technical Specification Table 3.6.3-
    1, ``Primary Containment Isolation Valves,'' since these valves are no 
    longer needed to support the steam condensing mode of the residual heat 
    removal (RHR) system and are being removed from the plant.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        With the prior deletion of the steam condensing mode of RHR and 
    the isolation of the high and low pressure interfaces, the three 
    pressure relief valves that are being removed from the plant have no 
    active function. Their passive function of maintaining system or 
    containment integrity will be fulfilled by blind flanges. Also, the 
    RHR and RCIC [reactor core isolation cooling] piping are provided 
    with overpressure protection from other pressure relief valves. 
    Therefore, the removal of these pressure relief valves does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The pressure relief valves that are being removed had two 
    primary functions. First,
    
    [[Page 13532]]
    
    they provided overpressure protection for the RHR and RCIC piping 
    during the steam condensing mode of RHR. Since the steam condensing 
    mode has been deleted from the plant, these valves no longer have 
    that function. Also, overpressure protection of the RHR and RCIC 
    piping is provided by other existing pressure relief valves. Second, 
    these valves maintained system or containment integrity. When the 
    pressure relief valves are removed from the plant, they will be 
    replaced with blind flanges or equivalent that will maintain system 
    or containment integrity. Therefore, the removal of the three 
    pressure relief valves does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        Since the steam condensing mode of RHR has been eliminated, the 
    three pressure relief valves have no active function. Their passive 
    function of maintaining system or containment integrity will be 
    fulfilled by blind flanges or equivalent. Also, overpressure 
    protection of RHR and RCIC piping is provided by other existing 
    pressure relief valves. Therefore, the removal of the three pressure 
    relief valves does not involve a significant reduction in a margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location:  Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: January 25, 1996
        Description of amendment request: The amendment proposes to revise 
    the allowed out-of-service times for single inoperable Emergency Diesel 
    Generators (EDGs) to accommodate on-line maintenance of the EDGs. In 
    addition, two line item changes are proposed: (1) to improve safety by 
    reducing EDG testing at power; and (2) to revise the ac power 
    requirements during cold shutdown or refueling modes to make the James 
    A. FitzPatrick (JAF) Technical Specifications consistent with the 
    Standard Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        a. EMERGENCY DIESEL GENERATOR LCO [Limiting Conditions for 
    Operation] AT POWER
        The proposed changes to the Technical Specifications will allow 
    longer Allowed Out of Service Times [AOTs] to perform necessary 
    repair and maintenance on individual Emergency Diesel Generators 
    while at power. This extended AOT will enhance scheduling of 
    preventive maintenance of individual EDGs without significantly 
    increasing the probability or consequences of an accident previously 
    evaluated. The risk evaluations contained in the JAF quantitative 
    analyses of the EDGs determined that the probability of an accident 
    by increasing the AOT for an individual EDG from 7 days to 14 days 
    is non-risk-significant. The primary reason for this low relative 
    risk is due to the designed redundancy and capability to respond to 
    an accident when a single diesel generator is out of service. LOCA 
    [loss-of-coolant accident] Analyses that assume the worst case line 
    break while an EDG is out of service indicate the plant can be 
    safely shut down with the remaining EDGs. Even if another EDG should 
    fail during the AOT, at least one Core Spray and one Residual Heat 
    Removal (RHR) Low Pressure Coolant Injection pump can provide the 
    required flow to bring the plant to safe shut down. Furthermore, 
    long term suppression pool and reactor shutdown cooling is provided 
    by any one of the three remaining RHR pumps for a single EDG out of 
    service or by two remaining RHR pumps assuming an additional EDG 
    failure during the AOT.
        Increasing the EDG AOT does not involve physical alteration of 
    any plant equipment and does not affect analysis assumptions 
    regarding functioning of required equipment designed to mitigate the 
    consequences of accidents. Further, the severity of postulated 
    accidents and resulting radiological effluent releases will not be 
    affected by the increased AOT for a single EDG.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. EMERGENCY DIESEL GENERATOR LCO DURING PLANT SHUTDOWN
        Changing the number of EDGs required during plant shutdown does 
    not involve physical alteration of any plant equipment and does not 
    affect analysis assumptions regarding functioning of required 
    equipment designed to mitigate the consequences of accidents. 
    Further, the severity of postulated accidents and resulting 
    radiological effluent releases will not be affected by the change in 
    the LCO during shutdown.
        c. EMERGENCY DIESEL GENERATOR SURVEILLANCE AT POWER OPERATION
        The proposed change to the Technical Specification will reduce 
    the required number of tests to be performed when an EDG or EDG 
    System is inoperable. This proposed change to TS requirements 
    addresses the concern of excessive testing that could result in EDG 
    wear which is counter-productive to safety in terms of equipment 
    degradation and availability. This change is consistent with Generic 
    Letter 93-05 guidance for implementing such recommendations. The 
    proposed Technical Specifications will not result in a change to the 
    design or operation of the facility, therefore, this change will not 
    result in a significant increase in the probability or consequences 
    of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        a. EMERGENCY DIESEL GENERATOR LCO AT POWER
        Extending the AOT for an individual EDG does not necessitate 
    physical alteration of the plant or changes in parameters governing 
    normal plant operation. Thus, this change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated for JAF plant.
        b. EMERGENCY DIESEL GENERATOR LCO DURING PLANT SHUTDOWN
        Changing the number of EDGs required during shutdown does not 
    necessitate physical alteration of the plant or changes in 
    parameters governing normal plant operation. Thus, this change does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated for JAF plant.
        c. EMERGENCY DIESEL GENERATOR SURVEILLANCE AT POWER OPERATION
        The proposed change does not change design, operation or the 
    testing process. The nature of this change precludes the possibility 
    of a new or different kind of accident. The proposed change to 
    complete the required action does not involve any hardware changes, 
    nor changes to the operation of the equipment nor does it change the 
    ability of the equipment to perform its intended function. 
    Performing the testing on an extended time cannot initiate any type 
    of accident.
        3. Involve a significant reduction in the margin of safety.
        a. EMERGENCY DIESEL GENERATOR LCO AT POWER
        As discussed above, the JAF quantitative evaluation determined 
    that the change in risk associated with extending the AOT for a 
    single EDG is non-risk-significant. In addition, the design provides 
    adequate redundancy for safe shut down during the AOT for a single 
    EDG out of service. This is supported by the LOCA analyses including 
    analyses for long term suppression pool and reactor shutdown 
    cooling.
        b. EMERGENCY DIESEL GENERATOR LCO DURING PLANT SHUTDOWN
        The margin of safety is not affected by changing the number of 
    EDGs required during shutdown. One offsite power source or one EDG 
    ensure the availability of the
    
    [[Page 13533]]
    
    required power to recover from postulated accident events during 
    shutdown. When the required number of operable systems is not met, 
    all work that could potentially initiate a postulated accident event 
    during shutdown is suspended.
        c. EMERGENCY DIESEL GENERATOR SURVEILLANCE AT POWER OPERATION
        The proposed change to Technical Specifications reduces testing 
    at reactor power. The overall effect is a net gain in plant safety 
    by avoiding the potential for unnecessary wear that could degrade 
    the EDGs at power. Implementation of these changes is consistent 
    with the guidance provided by the NRC in Generic Letter 93-05. The 
    proposed change to the EDG testing requirements does not reduce the 
    ability of the equipment to perform its intended safety function.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Ledyard B. Marsh
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
        Date of amendment request: January 30, 1996
        Description of amendment request: The proposed Technical 
    Specifications change will delete the requirement that oxygen 
    concentrations for both normal and transient conditions not exceed 
    saturation when the reactor coolant is below 250 degrees F. The 
    Technical Specifications change will also eliminate the surveillance 
    requirement for reactor coolant chemistry sampling of chloride, 
    fluoride, and oxygen concentration during maintenance activities when 
    fuel is removed from the reactor vessel and the Reactor Coolant System 
    (RCS) is drained below the reactor vessel flange regardless of whether 
    the upper internal and/or vessel heat are in place or not. 
    Administrative result of the changes being made, capitalize Technical 
    Specifications defined terms to maintain consistency within the 
    Technical Specifications, and the word ``degrees'' is spelled-out when 
    referring to the Fahrenheit temperature, rather than using the symbol.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of Surry Power Station in accordance 
    with the proposed changes will not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Since the RCS and the RHR [Residual Heat Removal] System are 
    drained when the RCS inventory is reduced below the reactor vessel 
    flange for maintenance or refueling activities, the concentrations 
    of chlorides and fluorides will not change. During these maintenance 
    or refueling activities, only controlled makeup to the RCS is 
    planned, and any planned or unplanned makeup to the RCS would be 
    detected by available level indication. Sampling for chloride and 
    fluoride concentrations in the RCS will be performed prior to 
    draining the system. Sampling of the reactor coolant for chloride 
    and fluoride concentrations will resume when the RCS is filled. The 
    chloride and fluoride concentrations will be known and will be 
    maintained consistent with the Technical Specification Limiting 
    Condition for Operation and Action Statements. Also, when the RCS 
    inventory is drained below the reactor vessel flange, the RCS is 
    vented and open to the containment building atmosphere with the 
    reactor coolant liquid considered oxygen saturated. Technical 
    Specification 3.1.F.4 allows normal and off-normal ``saturated'' 
    oxygen concentrations when reactor coolant temperature is below 250 
    degrees F. Consequently, sampling the reactor coolant for oxygen 
    concentration under these conditions is not required and the 
    Technical Specification Table 4.1-2B specified sampling frequency of 
    five (5) times per week is not necessary since the oxygen 
    concentration continues to remain in compliance with the Technical 
    Specification limit, measures are available and action can be taken 
    to correct the condition prior to any deleterious effect.
        Surry Technical Specifications 3.1.F.1 prohibits reactor coolant 
    temperature from exceeding 250 degrees F unless chloride, fluoride, 
    and oxygen concentrations are within specified limits. Therefore a 
    significant increase in the probability or consequences of an 
    accident previously evaluated does not exist.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The materials that are exposed to reactor coolant are corrosion 
    resistant. They were chosen for specific applications within the 
    system and for their compatibility with the reactor coolant. The 
    chemical composition of the reactor coolant will be maintained 
    within the specifications given within Technical Specification 
    3.1.F, Updated Final Safety Analysis Report Table 4.2-2, and 
    Technical Specification Table 4.1-2B. Because of the time dependent 
    nature of any adverse affects from chloride, fluoride, and oxygen 
    concentrations in excess of the Technical Specifications limits, 
    measures are available and can be taken to correct the condition 
    while the reactor is in a safe shutdown condition, prior to any 
    deleterious effect. No hardware modifications are involved. System 
    configuration and plant operations are not being changed. Therefore, 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated has not been created.
        (3) Involve a significant reduction in the margin of safety.
        This change does not involve a significant reduction in the 
    margin of safety since the chloride and fluoride concentrations are 
    maintained within their specified values prior to RCS drain down and 
    following refill. The time period during which the RCS inventory is 
    reduced below the reactor vessel flange and fuel is removed from the 
    vessel, is short and insignificant in terms of the parameters 
    necessary to initiate a corrosion concern. Existing Technical 
    Specifications Action Statements and Allowed Technical Specification 
    values for normal and off-normal concentrations of chlorides and 
    fluorides are not being changed. No hardware modifications are 
    involved. System configuration and plant operations are not being 
    changed. Surry Technical Specification 3.1.F.1 remains unaffected by 
    this change and continues to prohibit reactor coolant temperature 
    from exceeding 250 degrees F unless chloride, fluoride, and oxygen 
    concentrations are within specified limits.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219
        NRC Project Director: Eugene V. Imbro
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued
    
    [[Page 13534]]
    
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket No. 50-498, South Texas Project, Unit 1, Matagorda County, 
    Texas
    
        Date of amendment request: February 29, 1996
        Description of amendment request: The proposed amendment would 
    include the addition of Technical Specification 3.10.8 which would 
    allow a one-time only extension of the standby diesel generator (SDG) 
    allowed outage time for a cumulative 21 days on ``A'' train SDG. In 
    addition, it would also allow a one-time only extension of the allowed 
    outage time on ``A'' train essential cooling water loop for a 
    cumulative 7 days. This one-time only change would become effective on 
    April 10, 1996, and expire on May 15, 1996.Date of individual notice in 
    the Federal Register: March 8, 1996 (61 FR 9502)
        Expiration date of individual notice: April 8, 1996
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 1, 1995, as supplemented by letters 
    dated June 22, August 28, November 22, and December 19, 1995, and 
    January 4, January 8 (two letters), and January 23, 1996
        Description of amendment request: The proposed amendment would 
    provide a special test exception that would allow an extension of the 
    standby diesel generator (SDG) allowed outage time for a cumulative 21 
    days on each SDG once per fuel cycle, and it would also allow an 
    extension of the essential cooling water (ECW) loop allowed outage time 
    for a cumulative 7 days on each ECW loop once per fuel cycle. These 
    extended allowed outage times will be used to perform required 
    inspections and maintenance on the SDGs and the ECW system during power 
    operation.
        Date of individual notice in the Federal Register: February 8, 1996 
    (61 FR 4805)
        Expiration date of individual notice: March 11, 1996
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: March 1, 1996 (supersedes December 11, 
    1995, application)
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Section 4.7, ``Surveillance Requirements 
    for Primary Containment Automatic Isolation Valves.'' Specifically, the 
    proposed amendment would revise the replacement frequency of the seat 
    seals for the drywell and suppression chamber purge and vent valves 
    from every 5 years to every six operating cycles.
        Date of individual notice in the Federal Register: March 8, 1996 
    (61 FR 9504)
        Expiration date of individual notice: April 8, 1996
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: November 7, 1995, as 
    supplemented by letter dated January 17, 1996.
        Brief description of amendments: These amendments adopt the 
    improved Standard Technical Specifications (NUREG-1432) format and 
    content of Section 5.0, ``Design Features,'' as modified by approved 
    changes to the improved Standard Technical Specifications.
        Date of issuance: March 6, 1996
        Effective date: March 6, 1996, to be implemented within 45 days of 
    the date of issuance.
        Amendment Nos.: Unit 1 - Amendment No. 104; Unit 2 - Amendment No. 
    93; Unit 3 - Amendment No. 76
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65673) The January 17, 1996, supplemental letter provided clarifying 
    information and did not change the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated March 6, 1996.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location:  Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
    
    [[Page 13535]]
    
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: February 16, 1996
        Brief description of amendment: The amendment allows a one-time 
    extension for the performance of the trip actuating device operational 
    test for one of the safety injection manual initiation switches listed 
    in Technical Specification Table 4.3-2, Item 1a.Date of issuance: March 
    11, 1996
        Effective date: March 11, 1996
        Amendment No. 63
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: Yes (61 FR 7125). That notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by March 27, 1996, but indicated that if the Commission makes a 
    final no significant hazards consideration determination any such 
    hearing would take place after issuance of the amendment. The 
    Commission's related evaluation of the amendment, finding of exigent 
    circumstances, and final determination of no significant hazards 
    consideration is contained in a Safety Evaluation dated March 11, 1996
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois, Docket 
    Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 
    2, Will County, Illinois
    
        Date of application for amendments: January 11, 1996
        Brief description of amendments: The amendments revise the action 
    statements and allowed outage time for inoperability of one channel and 
    both channels of source range neutron flux instrumentation in Shutdown 
    Modes 3, 4, and 5.
        Date of issuance: March 15, 1996
        Effective date: March 15, 1996
        Amendment Nos.: 80, 80, 72, and 72
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3509) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 15, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: November 14, 1995, as 
    supplemented January 4, 1996 and February 29, 1996.
        Brief description of amendments: The amendments revise the 
    Technical Specifications to incorporate 10 CFR Part 50, Appendix J, 
    ``Primary Reactor Containment Leakage Testing for Water-Cooled Power 
    Reactors,'' Option B.
        Date of issuance: March 11, 1996 Effective date: Immediately, to be 
    implemented no later than June 30, 1996.
        Amendment Nos.: 110 and 95
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1995 (60 FR 
    62896) The January 4, 1996, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    March 11, 1996. No significant hazards consideration comments received: 
    No
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of application for amendment: September 20, 1995, as 
    supplemented December 18 and December 22, 1995.
        Brief description of amendment: The amendment allows a one-time 
    surveillance interval extension for certain 18-month surveillances 
    listed in new Technical Specification Tables 4.0.2-1 and 4.0.2-2. Date 
    of issuance: March 1, 1996
        Effective date:
        March 1, 1996, with full implementation within 90 days.
        Amendment No.: 106
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 27, 1995 (60 
    FR 58400). The December 18, 1995, letter corrected a typographical 
    error on one of the proposed TS pages and provided a corrected Table of 
    Contents page to reflect the addition of the new Tables. The December 
    22, 1995, letter provided additional information on the licensee's 
    review of historical plant drift data. This information was within the 
    scope of the original application and did not change the staff's 
    initial no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated March 1, 1996.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of application for amendments: November 10, 1995
        Brief description of amendments: The amendments revise the 
    Technical Specifications for containment systems to reflect the 
    adoption of the requirements of 10 CFR Part 50, Appendix J, Option B, 
    and the implementation of a performance-based containment leak-rate 
    testing program at the Edwin I. Hatch Nuclear Plant, Units 1 and 2.
        Date of issuance: March 6, 1996
        Effective date: As of the date of issuance to be implemented within 
    90 days
        Amendment Nos.: Unit 1 - 200 - Unit 2 - 141
        Facility Operating License Nos. DPR-57 and NPF-5. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65679) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 6, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
    
    [[Page 13536]]
    
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: December 5, 1995
        Brief description of amendment: The amendment revises the submittal 
    date for the Annual Exposure Data Report bringing Oyster Creek into 
    conference with 10 CFR 20.2206 and relaxes an overly restrictive 
    administrative requirement.
        Date of Issuance: March 4, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 183
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1629). The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated March 4, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: December 14, 1995
        Brief description of amendment: The amendment modifies Technical 
    Specification 3.4.2, ``Flow Control Valves (FCVs),'' by deleting 
    Surveillance Requirement (SR) 3.4.2.2, which required periodic 
    verification that the average rate of movement of each reactor 
    recirculation system FCV was limited to less than or equal to 11% per 
    second in the opening and closing directions. Due to a plant 
    modification, the requirement is not applicable.
        Date of issuance: March 11, 1996
        Effective date: March 11, 1996
        Amendment No.: 103
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1630) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 11, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: November 10, 1995 
    (AEP:NRC:0896X). This application superseded a request dated June 15, 
    1995 (AEP:NRC:0896V).
        Brief description of amendments: The amendments change the 18-month 
    emergency diesel generator surveillance test from a 24-hour run to an 
    8-hour run and add voltage and frequency measurement and power factor 
    monitoring.
        Date of issuance: March 11, 1996
        Effective date: March 11, 1996, with full implementation within 45 
    days
        Amendment Nos.: Unit 1 - 207, Unit 2 - 191
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65682) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 11, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: June 20, 1995, as supplemented 
    December 19, 1995.
        Brief description of amendments: The amendments relocate the fire 
    protection program elements from the Technical Specifications and 
    incorporate, by reference, the NRC-approved Fire Protection Program and 
    major commitments, including the fire hazards analysis, into the 
    Updated Final Safety Analysis Report. In addition, the amendments 
    revise the operating licenses to include the NRC's standard fire 
    protection license condition.
        Date of issuance: March 11, 1996
        Effective date: March 11, 1996, with full implementation within 180 
    days
        Amendment Nos.: Unit 1 - 208, Unit 2 - 192
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications and the operating licenses.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47620). The December 19, 1995, supplement clarified the license 
    conditions by providing specific approval dates for previous fire 
    protection safety evaluations. This information was within the scope of 
    the original application and did not change the staff's initial 
    proposed no significant hazards consideration determination.The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated March 11, 1996.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    MillstoneNuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: June 29, 1995
        Brief description of amendment: The amendment revises the Technical 
    Specifications to extend the surveillance schedule from 18 months to 
    each refueling interval (nominally 24 months) for specifications 
    4.6.4.2, 4.7.1.2.1.c, 4.7.3.b, 4.7.4.b,and 4.7.10.e. It also deletes 
    specification 4.6.4.2.a and the phrase ``during shutdown'' from these 
    specifications.Date of issuance: March 4, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 90 days.
        Amendment No.: 127
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 27, 1995 (60 
    FR 58402) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 4, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Pacific Gas and Electric Company, Docket No. 50-275, Diablo Canyon 
    Nuclear Power Plant, Unit No. 1, San Luis Obispo County, California
    
        Date of application for amendment: January 18, 1996
        Brief description of amendment: The amendment revises the combined 
    Technical Specifications (TS) for the Diablo Canyon Nuclear Power 
    Plant, Unit No. 1. TS 3.8.1.1, ``Electrical Power Systems - A.C. 
    Sources - Operating,'' is revised to allow operation of Unit 1 in Mode 
    3 (Hot Standby) during installation of a replacement non-vital 
    auxiliary transformer 11, for a one time
    
    [[Page 13537]]
    extension of up to 48 hours beyond the 72 hours allowed by TS 3.8.1.1, 
    Action Statement (a).
        Date of issuance: March 8, 1996
        Effective date: March 8, 1996
        Amendment No.: Unit 1 - Amendment No. 111
        Facility Operating License No. DPR-80: The amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1996 (61 FR 
    3737) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 8, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: December 27, 1995
        Brief description of amendments: The amendments revised the 
    combined Technical Specifications (TS) 3/4.6.1.1, Containment 
    Integrity; 3/4.6.1.2, Containment Leakage; 3/4.6.1.3, Containment Air 
    Locks; 3/4.6.1.6, Containment Structural Integrity; 3/4.6.3, 
    Containment Isolation Valves; their associated Bases; and adds 
    Specification 6.8.4 j., Containment Leakage Rate Testing Program to 
    implement the performance based leakage rate testing program as 
    permitted by 10 CFR Part 50, Appendix J, rather than paraphrasing the 
    requirements of the regulation. These changes will support the 
    implementation of the performance based testing of Option B to Appendix 
    J, for Type A, B, and C containment leakage rate testing and the 
    appropriate rescheduling of testing.
        Date of issuance: March 1, 1996 Effective date: March 1, 1996
        Amendment Nos.: Unit 1 - Amendment No. 110; Unit 2 - Amendment No. 
    109
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3502) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 1, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: April 13, 1994, as supplemented 
    December 6, 1995
        Brief description of amendment: The proposed changes revise the 
    Quality Assurance audit frequencies in the Hope Creek Technical 
    Specifications. These revisions will permit an audit frequency based on 
    performance and transfer subsequent control over the audit program to 
    the Updated Final Safety Analysis Report.
        Date of issuance: March 11, 1996
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment No.: 95
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29633) The December 6, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination nor the original Federal Register 
    notice.The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 11, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: April 13, 1994, as supplemented 
    December 6, 1995.
        Brief description of amendments: The proposed changes revise the 
    Quality Assurance audit frequencies in the Salem Unit Nos. 1 and 2 
    Technical Specifications. These revisions will permit an audit 
    frequency based on performance and transfer subsequent control over the 
    audit program to the Updated Final Safety Analysis Report.
        Date of issuance: March 11, 1996
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment Nos. 181 and 162
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29633) The December 6, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination nor the original Federal Register 
    notice.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 11, 1996No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: December 8, 1995 (TS 93-09)
        Brief description of amendments: The amendments revise the 
    setpoints and time delays for the auxiliary feedwater loss-of-power and 
    the 6.9-kilovolt shutdown board loss-of-voltage and degraded voltage 
    instruments.
        Date of issuance: March 1, 1996
        Effective date: March 1, 1996
        Amendment Nos.: 219 and 209
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    181) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 1, 1996.No significant hazards 
    consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: January 4, 1996 (TS 95-22)
        Brief description of amendments: The amendments change the 
    surveillance test frequency specified for the functional tests of the 
    containment, fuel storage pool, and control room radiation monitors 
    from monthly to quarterly.
        Date of issuance: March 4, 1996
        Effective date: March 4, 1996
        Amendment Nos.: 220 and 210
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3503)
    
    [[Page 13538]]
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated Macrh 4, 1996.No significant hazards 
    consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: January 16, 1996, and supplement 
    dated March 1, 1996
        Brief description of amendment: This amendment approves that part 
    of the request that defers the drywell bypass leakage test during the 
    current refueling outage. The remainder of the licensee's request is 
    still under NRC staff review.
        Date of issuance: March 8, 1996
        Effective date: March 8, 1996
        Amendment No. 82
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1996 (61 FR 
    3951) The March 1, 1996, supplemental letter was clarifying in nature 
    and did not affect the initital no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 8, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: December 9, 1994, as 
    supplemented by letters dated September 13, 1995, and February 9, 1996.
        Brief description of amendment: The amendment revises Technical 
    Specifications (TS) 4.3.2.2, TS 4.7.1.2.1, and the Bases for TS 3/4 
    7.1.2 to decrease the frequency of auxiliary feedwater pump testing, 
    remove inconsistencies in testing requirements for the turbine-driven 
    auxiliary feedwater pump, and clarify performance parameters in the TS 
    Bases.
        Date of issuance: March 11, 1996
        Effective date: March 11, 1996, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 108
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6314). The September 13, 1995, and February 9, 1996, supplemental 
    letters provided additional clarifying information and did not change 
    the original no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated March 11, 1996.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: September 19, 1995
        Brief description of amendments: The amendments revised the maximum 
    allowable power range neutron flux high setpoints for operation with 
    inoperable main steam safety valves.
        Date of issuance: March 6, 1996
        Effective date: March 6, 1996
        Amendment Nos.: 199 and 180
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: October 25, 1995 (60 FR 
    54724) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 6, 1996No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: November 22, 1995
        Brief description of amendment: The amendment replaces the 
    Technical Specification (TS) requirements associated with the boron 
    dilution mitigation system (BDMS) with alarms, indicators, procedures 
    and controls to allow proper resolution of potential boron dilution 
    events.
        Date of issuance: March 1, 1996
        Effective date: March 1, 1996, to be implemented prior to the 
    startup from the eighth refueling outage.
        Amendment No.: 96
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3503) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 1, 1996.No significant hazards 
    consideration comments received: No. Local Public Document Room 
    locations: Emporia State University, William Allen White Library, 1200 
    Commercial Street, Emporia, Kansas 66801 and Washburn University School 
    of Law Library, Topeka, Kansas 66621
        Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
        Date of amendment request: December 20, 1995, as supplemented by 
    letter dated February 8, 1996.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to reflect the approval of the use of 10 CFR Part 50, 
    Appendix J, Option B for the Wolf Creek Generating Station containment 
    leakage rate test program.
        Date of issuance: March 1, 1996
        Effective date: March 1, 1996, to be implemented prior to startup 
    from the eighth refueling outage.
        Amendment No.: 97
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3504) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 1, 1996.No significant hazards 
    consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: December 13, 1995
        Brief description of amendment: The amendment revises the minimum 
    and maximum flow requirements for the centrifugal charging pumps (CCPs) 
    and safety injection pumps (SIPs) specified in Technical Specification 
    (TS) Surveillance Requirement 4.5.2.h. Specifically, the amendment (1) 
    decreases the minimum limits on the sum of the injection line flow 
    rates,
    
    [[Page 13539]]
    excluding the highest flow rate, from 346 gallons per minute (gpm) to 
    330 gpm for the CCPs and from 459 gpm to 450 gpm for the SIPs, and (2) 
    revises the maximum pump flow rate for the SIPs from 665 to 670 gpm, 
    but retains the CCPs maximum pump flow rate at its current value of 556 
    gpm.Date of issuance: March 5, 1996
        Effective date: March 5, 1996, to be implemented prior to startup 
    from the eighth refueling outage.
        Amendment No.: 98
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1639) The February 5, 1996, supplemental letter provided additional 
    clarifying information and did not change the original no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    March 5, 1996.No significant hazards consideration comments received: 
    No. Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By April 26, 1996, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be
    
    [[Page 13540]]
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: March 6, 1996
        Brief description of amendment: This amendment revises TS 3/4 5.2, 
    ECCS SUBSYSTEMS - T avg greater than or equal to 280 deg.F by 
    modifying Surveillance Requirement 4.5.2.b to defer venting of the 
    Emergency Core Cooling System flow path which does not have manual 
    venting capability until the tenth refueling outage.
        Date of issuance: March 7, 1996
        Effective date: March 7, 1996
        Amendment No: 208
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendments, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 7, 1996.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
        Dated at Rockville, Maryland, this 20th day of March 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga, Director,
    Division of Reactor Projects - I/II,Office of Nuclear Reactor 
    Regulation
    [Doc. 96-7259 Filed 3-26-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
03/27/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-7259
Dates:
March 6, 1996, to be implemented within 45 days of the date of issuance.
Pages:
13521-13540 (20 pages)
PDF File:
96-7259.pdf