X94-20330. Biweekly Notice Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 61 (Wednesday, March 30, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-20330]
    
    
    [[Page Unknown]]
    
    [Federal Register: March 30, 1994]
    
    
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    UNITED STATES NUCLEAR REGULATORY COMMISSION
    
     
    
    Biweekly Notice Applications and Amendments to Facility Operating 
    Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 7, 1994, through March 18, 1994. The 
    last biweekly notice was published on March 16, 1994.
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room P-223, Phillips Building, 7920 Norfolk Avenue, 
    Bethesda, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies 
    of written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By April 29, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, Unit 
    Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendment requests: February 18, 1994
        Description of amendment request: The proposed amendment would 
    modify Technical Specification (TS) Figure 3.2-1, ``REACTOR COOLANT 
    COLD LEG vs CORE POWER LEVEL,'' of TS 3/4.2.6, ``REACTOR COOLANT COLD 
    LEG TEMPERATURE,'' for Units 1 and 3 to include the cold leg 
    temperature between 552 deg.F and 562 deg.F at core power levels 
    between 90 percent and 100 percent within the AREA OF ACCEPTABLE 
    OPERATION. Also, the proposed amendment would modify TS 3/4.1.1.4, 
    ``MINIMUM TEMPERATURE FOR CRITICALITY,'' and BASES 3/4.1.1.4, ``MINIMUM 
    TEMPERATURE FOR CRITICALITY,'' for all units to allow the minimum 
    temperature for criticality to be established at 545 deg.F, rather than 
    the current value of 552 deg.F, to establish the surveillance 
    temperature at 552 deg.F, rather than the current 557 deg.F, and to 
    clarify the BASES for this TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis about the issue of no significant hazards 
    consideration, which is presented below:
        Standard 1 -- Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        This amendment does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    analyses performed confirmed that the existing safety analysis for 
    cycle 5 of all three PVNGS [Palo Verde Nuclear Generating Station] 
    units remains valid for a 10 deg.F reduction in RCS [reactor coolant 
    system] temperature.
        Standard 2 -- Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        This amendment does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. The 
    analyses performed demonstrated that the current licensing basis 
    analyses results remain valid with a 10 deg.F reduction in RCS [reactor 
    coolant system] temperature, and that the safety system settings remain 
    unchanged.
        Standard 3 -- Involve a significant reduction in a margin of 
    safety.
        This amendment request will not involve a significant reduction in 
    a margin of safety. There is no reduction in the margin of safety since 
    the changes apply only to the reactor coolant cold leg temperature and 
    the minimum temperature for criticality, the safety analyses have been 
    reevaluated (and reperformed where necessary) using the new 
    temperature, and the results remain valid. All other safety limits and 
    safety system settings remain unchanged. Therefore, there is no 
    reduction in any margin of safety.
        The NRC staff has reviewed the licensees' analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
        Attorney for licensees: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: Theodore R. Quay
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: February 4, 1994
        Description of amendment request: The proposed amendment revises 
    the Action Statement of Technical Specification 3.6.5, Vacuum Relief 
    System, to require that in Modes 1-4 with one vacuum relief system 
    inoperable the system be restored to operable status within seventy-two 
    hours or be in at least hot standby within the next six hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment does not physically alter the plant in 
    any manner. The proposed amendment does not introduce any new 
    equipment nor does it require any existing equipment or systems to 
    perform a different type of function than they are currently 
    designed to perform. The proposed amendment to Technical 
    Specification 3.6.5 allows additional time to restore an inoperable 
    containment vacuum relief system to operable status. Changing the 
    completion time to seventy-two hours remainsquite conservative for 
    this non-ESF system since a seventy-two hour restoration time is 
    specified for two-train ESF systems which mitigate Final Safety 
    Analysis Report (FSAR) Chapter 15 accidents. The CVRS [containment 
    vacuum relief system] is designed to protect the structural 
    integrity of containment during an inadvertent actuation of the 
    containment spray system, which is not an FSAR Chapter 15 accident. 
    Therefore, there would be no increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment does not introduce any new equipment nor 
    does it require any existing equipment or systems to perform a 
    different type of function than they are currently designed to 
    perform. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed amendment to Technical Specification 3.6.5 allows 
    additional time to restore an inoperable containment vacuum relief 
    system to operable status. Changing the completion time to seventy-
    two hours remains conservative since a seventy-two hour restoration 
    time is specified for two-train ESF systems which mitigate FSAR 
    Chapter 15 accidents. The CVRS is designed to protect the structural 
    integrity of containment during an inadvertent actuation of the 
    containment spray system, which is not an FSAR Chapter 15 accident. 
    Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety as defined in the Technical 
    Specifications of FSAR.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602
        NRC Project Director: S. Singh Bajwa
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: February 24, 1994
        Description of amendment request: The proposed amendments would 
    provide surveillance requirements for a planned modification to the 
    Keowee emergency power generators' underground power path breaker 
    closing logic. The planned modification would provide an automatic 
    close feature for the underground path breakers under certain specified 
    conditions. The modification is needed to correct a design deficiency 
    which resulted in a single failure vulnerability when both Keowee units 
    are in their normal alignment. The single failure vulnerability is 
    being prevented by means of administrative controls pending 
    implementation of a permanent corrective action. The proposed 
    amendments would add an annual operability test to Technical 
    Specification 4.6, Emergency Power Periodic Testing, of the automatic 
    close feature.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated:
        The Keowee Hydro units provide the main source of emergency 
    power for the Oconee Nuclear units, but they are not accident 
    initiators. The FSAR [Final Safety Analysis Report] Loss of Electric 
    Power Accident assumes two types of events: (1) Loss of load (unit 
    trip) and (2) Loss of all system and station power. The changes 
    performed by the modification that added the automatic closure 
    circuitry do not increase the likelihood of either. Also, the 
    modifications to the Keowee operating logic will not adversely 
    affect the ability to mitigate LOOP [Loss of Offsite Power], LOCA 
    [Loss of Coolant Accident], and LOCA/LOOP accidents as described in 
    the FSAR. The loss of all station power accident analysis 
    assumptions are still valid. This modification has no adverse impact 
    on the ability of the Keowee Units to satisfy their design 
    requirements to achieving rated speed and voltage within 23 seconds 
    of receipt of an emergency start signal.
        The surveillance change that is included in [the] amendment 
    request is provided to assure the availability of the electrical 
    power systems for mitigation of Design Basis Accidents (DBAs). As 
    described within the technical justification [from the licensee's 
    application], the Keowee breaker circuitry was modified to allow the 
    Keowee Unit that is aligned to the overhead power path to 
    automatically close to the underground power path if the postulated 
    fault occurs. The surveillance change is an additional restriction 
    not presently included in the Technical Specifications. [The] 
    amendment will ensure the operability of the Keowee Unit ACB [Air 
    Circuit Breaker] automatic close feature and will assure that proper 
    testing requirements are maintained.
        Based on the above and the technical justification provided in 
    [the amendment application], there is no significant increase in the 
    probability of a DBA as a result of this change, nor is there a 
    significant increase in the consequences of a DBA as a result of 
    this change since the proposed amendment assures the availability of 
    the electrical power system.
        (2) Create the possibility of a new or different kind of 
    accident from any kind of accident previously evaluated:
        The proposed change makes physical changes to the plant 
    configuration. However, the modification simply changes the Keowee 
    control logic to remove the possibility of a certain postulated 
    failure from causing a loss of emergency power to the Oconee nuclear 
    units. The Keowee emergency power systems will remain operable and 
    available to mitigate accidents. Operation of ONS [Oconee Nuclear 
    Station] in accordance with [the] Technical Specifications will not 
    create any failure modes not bounded by previously evaluated 
    accidents. Consequently, this change will not create the possibility 
    of a new or different kind of accident from any kind of accident 
    previously evaluated.
        (3) Involve a significant reduction in a margin of safety:
        Margins of safety associated with [the] Technical Specifications 
    have been evaluated. No safety or design limits are adversely 
    affected, so margins of safety as defined in the bases to any 
    Technical Specifications are not reduced as a result of the Keowee 
    modification. The design basis of the auxiliary electrical system is 
    to supply the required ES [Engineered Safeguards] loads of one Unit 
    and safe shutdown loads of the other two units. The Technical 
    Specification amendment includes an additional surveillance 
    restriction not presently included in the Technical Specifications. 
    The proposed amendment assures the continued availability of the 
    electrical power systems; thus preserving the existing margin of 
    safety. Therefore, there will be no significant reduction in any 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews, Director
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: September 7, 1993, as supplemented 
    February 8, 1994
        Description of amendment request: The proposed amendment would 
    revise the Physical Security Plan (PSP).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        The accident mitigation features of the plant are not affected by 
    the proposed compensatory measures for protecting the site during 
    periods when security systems are degraded and therefore no decrease 
    occurs in the effectiveness of the security program to protect against 
    radiological sabotage or increased risk to the public health and 
    safety. This is due to continued compliance with existing regulatory 
    requirements and other commitments within the security plan. These 
    changes have no impact on the design basis security threat and 
    accordingly do not create the possibility of a new or different kind of 
    accident. New systems, modes of equipment operation, failure modes or 
    other plan situations are not introduced by these changes. The proposed 
    changes allow flexibility for the use of compensatory measures and do 
    not change any safety limits, LCOs, or surveillance requirements on 
    equipment to operate the plant.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: February 14, 1994
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TSs) to reflect changes that have 
    been made to 10 CFR Part 20 AND 10 CFR 50.36a.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed revisions to the liquid and gaseous concentration 
    release rate limits will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated 
    because there will be no change in the types and amounts of 
    effluents that will be released, nor will there be an increase in 
    individual or cumulative occupational radiation exposures.
        The administrative changes for definitions, terminology, 
    paragraph references, and record keeping requirements are necessary 
    so that the Waterford 3 Technical Specifications will remain 
    consistent with the revised federal regulations (i.e., 10CFR20 and 
    10CFR50.36a). Record retention and reporting requirements will 
    continue to meet NRC regulations. These changes are administrative 
    in nature and do not affect plant hardware or operation.
        Restricting access to high radiation areas via guards rather 
    than locked doors provides operational flexibility while continuing 
    to meet the underlying intent of precluding unauthorized access.
        Therefore, the proposed changes will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        Changes to the liquid and gaseous concentration limits are 
    necessary to provide adequate operational flexibility. Operational 
    history at Waterford 3 has demonstrated that the use of 
    concentration values associated with the old 10CFR20.106 
    requirements has resulted in calculated maximum individual doses to 
    a member of the public that are small percentages of the limits of 
    10CFR50, Appendix I. The proposed revisions will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated because the revisions will not change the types 
    and amounts of effluent that will be released.
        The administrative changes for definitions, terminology, 
    paragraph references, and record keeping are necessary so that the 
    Technical Specifications will remain consistent with the revised 
    federal regulations (i.e., 10CFR20 and 10CFR50.36a). Record 
    retention and reporting requirements will continue to meet NRC 
    regulations. These changes are administrative in nature and do not 
    affect plant hardware or operation.
        Restricting access for ALARA [as low as reasonably achievable] 
    with guards rather than locked doors will continue to meet the 
    underlying intent of the TS. These changes do not involve plant 
    hardware or operation.
        Therefore, the proposed changes will not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        The proposed revisions do not involve any changes in the types 
    or increases in the amounts of effluents released off site. The 
    methodology used to control radioactive effluents and calculate 
    effluent monitor setpoints will result in the same effluent release 
    rate as the current methodology. The basic requirements for TS 
    concerning effluent releases (10CFR50.36a) indicate that compliance 
    with TS will keep average annual release to small percentages of 
    10CFR20 limits. For liquid effluent releases, the annual dose of 500 
    mrem, that is the bases for the concentrations in the new 10CFR20. 
    The 50.36a requirements further indicate that operational 
    flexibility is allowed, compatible with considerations of health and 
    safety, which may temporarily result in release higher than such 
    small percentages, but still within the limits specified in the old 
    10CFR20.106 that references Appendix B maximum permissible 
    concentrations (MPCs). For gaseous effluent releases, the limits 
    associated with the gaseous release rate TS will be maintained at 
    the current instantaneous dose rate limits. Compliance with the 
    limits of the new 10CFR20.1301 will be demonstrated by operating 
    within the limits of 10CFR50, Appendix I, and 40CFR190. The revision 
    will not change the types and amounts of effluent that will be 
    released.
        The administrative changes for definitions, terminology, 
    paragraph references, and record keeping are necessary so that the 
    Technical Specifications will remain consistent with the revised 
    federal regulations (i.e., 10CFR20 and 10CFR50.36a). Record 
    retention and reporting requirements will continue to meet NRC 
    regulations. These changes are administrative in nature and do not 
    affect plant hardware or operation.
        Controlling access to high radiation areas for ALARA can be 
    performed effectively by guards in place of locked doors. These 
    changes do not involve plant hardware or operation.
        Therefore, the proposed changes will not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, et al., Docket No. 50-335, St. 
    Lucie Plant, Unit No. 1, St. Lucie County, Florida
    
        Date of amendment request: February 22, 1994
        Description of amendment request: The proposed amendment modifies 
    the minimum stored borated water inventory requirements for Operational 
    Modes 1 through 4 by revising Figure 3.1-1 and Limiting Condition for 
    Operation (LCO) 3.1.2.8 of the unit Technical Specifications (TS). The 
    associated bases for TS 3/4.1.2 are also revised to reflect the 
    bounding borated water makeup volumes, as a function of boric acid 
    concentration, which define the proposed inventory requirements. The 
    proposed amendment will significantly improve operational flexibility 
    with no risk to plant safety and will provide for consistency of 
    operation between the two St. Lucie units.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Pursuant to 10 CFR 50.92, a determination may be made that a 
    proposed license amendment involves no significant hazards 
    consideration if operation of the facility in accordance with the 
    proposed amendment would not: (1) involve a significant increase in 
    the probability or consequences of an accident previously evaluated; 
    or (2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or (3) involve a significant 
    reduction in a margin of safety. Each standard is discussed as 
    follows:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendment will reduce the minimum borated water 
    inventory required to be stored in the Boric Acid Makeup Tanks 
    (BAMT) during unit operation in Modes 1 through 4. The reduction in 
    BAMT inventory will not affect any equipment postulated to 
    malfunction in the Updated Final Safety Analysis Report (UFSAR) to 
    initiate an accident nor will it impact the operation of any other 
    equipment whose malfunction could adversely affect safety-related 
    structures, systems, or components. Credit is not taken for boron 
    addition to the Reactor Coolant System from the BAMTs for purposes 
    of reactivity control in accidents analyzed in the UFSAR. The 
    minimum required capability to achieve and maintain safe shutdown 
    for such events has not been altered. Therefore, operation of the 
    facility in accordance with the proposed amendment will not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The reduction in minimum required BAMT inventory does not change 
    the boration system function, configuration, operation, or design 
    basis as described in the UFSAR. The proposed change does not alter 
    the modes of plant operation and does not affect the operation of 
    safety-related structures, systems, or components. Therefore, 
    operation of the facility in accordance with the proposed amendment 
    would not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The reduced BAMT minimum inventory requirements are defined by 
    analyses that utilize an approved plant cooldown scenario and 
    conservative physics parameters representative of the present and 
    future planned reactor core designs for St. Lucie Unit 1. The 
    analytical methodology employed to determine the revised inventory 
    requirements is the same as that used to establish the existing 
    inventory requirements. The existing reactivity control Limiting 
    Conditions for Operation (LCO) related to safe shutdown margins and 
    redundant boron flow paths have not been altered. Sufficient 
    quantities of borated water will continue to be stored in the BAMTs 
    to assure compliance with these LCOs during the prescribed plant 
    operating modes. Therefore, operation of the facility in accordance 
    with the proposed amendment would not involve a significant 
    reduction in a margin of safety.
        Based on the discussion presented above and on the supporting 
    Evaluation of Proposed TS Changes, FPL has concluded that this 
    proposed license amendment involves no significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: Harold F. Reis, Esquire, Newman and 
    Holtzinger, 1615 L Street, NW, Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: February 18, 1994
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications (TS) by deleting 
    the frequencies specified for audits performed under the cognizance of 
    the Company Nuclear Review Board (CNRB). The periodicity of the audits 
    for these activities will be controlled as described in the licensee's 
    Topical Quality Assurance Report (FPLTQAR), wherein the minimum audit 
    frequency for any activity is established as biennial unless the audit 
    is otherwise required to be performed more frequently by the TS, Code 
    of Federal Regulations, or other licensing commitments. Periodic audits 
    of selected aspects of operational phase activities are performed with 
    a frequency commensurate with safety significance. During the interval 
    between the periodic audits, continuing performance evaluations are 
    conducted of activities important to plant safety.
        In addition, the licensee proposes to revise the TS in accordance 
    with Generic Letter 93-07. Generic Letter 93-07, ``Modifications of the 
    Technical Specifications Administrative Control Requirements for 
    Emergency and Security Plans,'' issued December 28, 1993, provided 
    guidance for changes to the TS to remove the audit of the emergency and 
    security plans and implementing procedures from the list of 
    responsibilities of the company nuclear audit and review group. The 
    basis of this change is that Parts 50 and 73 of Title 10 of the Code of 
    Federal Regulations (10 CFR) include provisions that are sufficient to 
    address these requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments relocate the administrative control 
    criteria for minimum audit frequencies from the facility TS to the 
    FPL Quality Assurance (QA) Program. The QA Program is described in 
    the FPL Topical Quality Assurance Report pursuant to 10 CFR 50, 
    Appendix B. In addition, the proposed amendments in accordance with 
    Generic Letter 93-07, changes the TS to remove the audit of the 
    emergency and security plans and implementing procedures from the 
    list of responsibilities of the Company Nuclear Review Board. The 
    changes being proposed are administrative in nature and do not 
    affect assumptions contained in plant safety analyses, the physical 
    design and/or operation of the plant, nor do they affect the TS that 
    preserve safety analysis assumptions. Therefore, operation of the 
    facility in accordance with the proposed amendments would not affect 
    the probability or consequences of an accident previously analyzed.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The changes being proposed are administrative in nature and will 
    not change the physical plant or the modes of operation defined in 
    the Facility License. The change does not involve the addition or 
    modification of equipment nor does it alter the design or operation 
    of plant systems. Therefore, operation of the facility in accordance 
    with the proposed amendments would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The changes being proposed are administrative in nature and do 
    not alter the bases for assurance that safety-related activities are 
    performed correctly or the basis for any TS that is related to the 
    establishment of or maintenance of a safety margin. Therefore, 
    operation of the facility in accordance with the proposed amendments 
    would not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: Harold F. Reis, Esquire, Newman and Holtzer, 
    P.C., 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Unit 1, 
    Matagorda County, Texas
    
        Date of amendment request: March 14, 1994
        Description of amendment request: The licensee proposes to make a 
    change to the technical specifications to add a new Limiting Condition 
    For Operation (LCO), 3.0.6. LCO 3.0.6 will allow equipment removed from 
    service or declared inoperable to comply with actions to be returned to 
    service, under administrative controls, solely to perform testing. The 
    new LCO will permit non-compliance with the applicable Action statement 
    to perform the post-maintenance and surveillance testing required to 
    demonstrate the operability of the equipment being returned to service 
    or the operability of other equipment.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The implementation of LCO 3.0.6 will allow the orderly and 
    judicious return to service of inoperable equipment. This LCO will 
    permit equipment removed from service to comply with required actions 
    to be returned to service under administrative controls to verify the 
    component or system will perform its safety function. The 
    administrative controls will ensure the time involved will be limited 
    to only the time required to demonstrate the component or system's 
    operability. The implementation of this new LCO will provide an 
    acceptable method of testing technical specification equipment prior to 
    its return to operable service following required maintenance. These 
    actions will ensure that the equipment being returned to service is 
    capable of performing its designed safety function prior to being 
    declared operable. Therefore, this action will ensure the probability 
    or consequences of an accident previously evaluated are not 
    significantly increased.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The equipment is only being tested in its designed configuration or 
    being returned to service to allow testing of another component or 
    system. Therefore, the use of this new LCO will not result in a new or 
    different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    the margin of safety.
        The use of the new LCO will only allow the return to service of 
    equipment that is expected to operate as designed. The use of the LCO 
    will be limited to the performance of testing on the equipment being 
    returned to service or on other equipment that is dependent on the 
    equipment being returned to service. This testing is limited to post-
    maintenance testing and the testing necessary to prove operability. 
    Since the equipment will be controlled by administrative requirements 
    that will ensure all necessary actions are taken, this change does not 
    involve a significant reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton Texas 77488
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, NW, Washington, DC 20036
        NRC Project Director: Suzanne C. Black
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of amendment requests: February 22, 1994
        Description of amendment requests: The proposed amendments would 
    modify the technical specifications to reduce surveillance requirements 
    for testing during power operation. This modification was proposed to 
    licensees in NRC Generic Letter 93-05, ``Line Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operation.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1
        Although the surveillance requirements are lessened by these 
    proposed changes, the changes are consistent with those found 
    acceptable by the NRC in Generic Letter 93-05. The proposed changes 
    have been determined to be compatible with our plant operating 
    experience. Based on these considerations, it is concluded that the 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Criterion 2
        The proposed changes do not involve physical changes to the 
    plant or changes in plant operating configuration. The changes only 
    involve frequency of testing required to be performed. The changes 
    are consistent with those found to be acceptable by the NRC in 
    Generic Letter 93-05. Thus, it is concluded that the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Criterion 3
        Although the surveillance requirements are lessened by these 
    proposed changes, the changes are consistent with those found 
    acceptable by the NRC in Generic Letter 93-05. The proposed changes 
    have been determined to be compatible with our plant operating 
    experience. Based on these considerations, it is concluded that the 
    changes do not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Ledyard B. Marsh
    
    Indiana Michigan Power Company, Docket No. 50-316, Donald C. Cook 
    Nuclear Plant, Unit No. 2, Berrien County, Michigan
    
        Date of amendment request: February 15, 1994
        Description of amendment request: The proposed amendment would 
    delete from the Technical Specifications the operational and 
    surveillance requirements for the turbine overspeed protection system. 
    The licensee intends to continue testing of the overspeed protection 
    system as part of plant procedures.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (a) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed amendment does not involve a significant increase 
    in the probability or consequences for an accident previously 
    evaluated. The proposed deletion of the turbine overspeed protection 
    T/S [technical specification] will not significantly change the 
    surveillance tests on the Unit 2 turbine. The surveillance schedule 
    and tests will be under administrative procedures outside of the TSs 
    similar to that of Unit 1 and will be in line with operating 
    experience at Cook Nuclear Plant and applicable industry experience. 
    The Unit 2 turbine is now operating in its ninth operating cycle 
    with over 90,000 hours of operation. Turbine overspeed protection 
    surveillance results have been very good since unit startup in 1978. 
    In 1983, a wear problem was found with the overspeed plungers. 
    Replacement plungers were installed. Then in 1988, these plungers 
    were replaced with parts having stellited (hardened) surfaces. There 
    have been no subsequent problems. Our expectation is that the 
    turbine overspeed protection system will remain available to perform 
    its function of preventing excessive turbine overspeed. Lastly, the 
    STS [Standard Technical Specifications] developed by the MERITS 
    program in NUREG-1431 do not include a T/S for turbine overspeed 
    protection. The omission of an overspeed protection T/S in NUREG-
    1431 indicates that a T/S is not needed to ensure an adequate level 
    of safety for a nuclear facility. This view is supported by WCAP 
    11618 which uses the NRC's ``Interim Policy Statement Criteria'' to 
    evaluate the need for a turbine overspeed protection T/S and 
    concludes that it is not needed. For these reasons, we believe that 
    deleting the turbine overspeed protection T/S will not significantly 
    increase the probability or consequences of an accident previously 
    evaluated.
        (b) Create the possibility of a new or different kind of 
    accident from any previously analyzed.
        The proposed amendment does not create the possibility of a new 
    or different kind of accident from any previously evaluated. This 
    request to delete the turbine overspeed protection T/S eliminates a 
    control on the surveillance testing of the Unit 2 turbine. The 
    design function of the turbine overspeed protection and the 
    operation of the turbine/generator remain the same. The operating 
    history of the Unit 2 surveillance results to date and our continued 
    testing support the view that the turbine overspeed protection will 
    remain available. For these reasons, we believe that the proposed 
    changes will not create the possibility of a new or different kind 
    of accident from any previously analyzed.
        (c) Involve a significant reduction in a margin of safety.
        The proposed amendment does not involve a significant reduction 
    in the margin of safety. Turbine overspeed protection surveillance 
    results have been excellent since 1983. The years of operating data 
    well within acceptance criteria on Unit 2 turbine overspeed 
    protection provide ample evidence that there is no significant 
    degradation of the system to perform its function. The reliability 
    of the overspeed protection was improved by the replacement of the 
    plungers with parts having stellited surfaces. The surveillance 
    schedule and tests will be based on operating experience at Cook 
    Nuclear Plant and applicable industry experience. Surveillance 
    testing will continue under an administrative program outside of 
    TSs. Thus the turbine overspeed protection is expected to remain 
    available. Also by eliminating this T/S we will be reducing the 
    potential for shutting down the unit because of difficulties 
    performing this T/S surveillance unrelated to the functionality of 
    the valves and overspeed trip protection. Lastly, the STS developed 
    by the MERITS program in NUREG-1431 do not include a T/S for turbine 
    overspeed protection. The omission of an overspeed protection T/S in 
    NUREG-1431 indicates that a T/S is not needed to ensure an adequate 
    level of safety for a nuclear facility.
        This view is supported by WCAP 11618 which uses the NRC's 
    ``Interim Policy Statement Criteria'' to evaluate the need for a 
    turbine overspeed protection T/S and concludes that it is not 
    needed. For these reasons, we believe that the turbine overspeed 
    protection system will remain operable and so this proposed 
    amendment does not involve a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Ledyard B. Marsh
    
    Indiana Michigan Power Company, Docket No. 50-316, Donald C. Cook 
    Nuclear Plant, Unit No. 2, Berrien County, Michigan
    
        Date of amendment request: February 22, 1994
        Description of amendment request: The proposed amendment would 
    revise the reactor coolant system heatup and cooldown curves in the 
    Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes to the P-T [pressure-temperature] curves 
    are being updated as a result of the Unit 2 Capsule U analysis, 
    WCAP-13515. The analysis was required per the removal schedule 
    established in Table 4.4-5 of the Cook Nuclear Plant Technical 
    Specifications. The analysis was performed based on guidance from R/
    G 1.99 [Regulatory Guide 1.99, ``Radiation Embrittlement of Reactor 
    Vessel Materials''], Revision 2. The change only involves a revised 
    time frame for material qualification from 12 EFPY [effective full-
    power years] to 15 EFPY as supported by the aforementioned 
    Westinghouse analysis. Therefore, we conclude that the changes will 
    not involve a significant increase in the probability or 
    consequences of a previously evaluated accident, nor will the 
    changes involve a significant reduction in a margin of safety.
        (2) Create the possibility of a new or different kind of 
    accident from any previously analyzed.
        The proposed changes do not involve any physical modifications 
    to the plant. Therefore, the changes should not create the 
    possibility of a new or different kind of accident from any 
    previously analyzed or evaluated.
        (3) Involve a significant reduction in a margin of safety.
        See the response to (1) above.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Ledyard B. Marsh
    
    Long Island Power Authority, Docket No. 50-322, Shoreham Nuclear 
    Power Station, Unit 1 (SNPS), Wading River, New York
    
        Date of application for amendment: Amendment No. 11, November 4, 
    1993 (Reference LSNRC-2115)
        Brief description of amendment: This license amendment request 
    (LSNRC-2115) proposes to delete from the Possession-Only License (POL) 
    the requirements associated with the safe storage and handling of 
    irradiated fuel, the accompanying Appendix A of SNPS Technical 
    Specifications, and Appendix B of SNPS Environmental Protection Plan 
    (non-radiological). This proposed amendment will update the SNPS POL to 
    reflect the status of the facility after irradiated fuel removal from 
    the site. SNPS License Condition No. 3 prohibits this amendment from 
    being implemented until all the fuel has been removed from SNPS, and 
    the licensee has certified to the NRC that all the fuel has been 
    removed.
        Basis for the proposed no significant hazards consideration 
    determination: In accordance with the requirements and standards in 10 
    CFR 50.92(c), the licensee has provided an analysis of the issues 
    related to the no significant hazards consideration.
        The licensee's analysis of the issues related to no significant 
    hazards consideration are presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes will become effective after the fuel and 
    its related hazards are removed from the site.
        Therefore, the proposed changes will update the SNPS license to 
    reflect the facility status after the removal of irradiated fuel. 
    This action will not increase the probability or consequences of any 
    accident previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes will update the license by deleting 
    requirements which will no longer apply to SNPS and will not have an 
    adverse impact on the operation of the remaining plant systems and 
    components.
        Therefore, the proposed change does not create the possibility 
    for an accident or malfunction different from any previously 
    analyzed.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed change will update the license to reflect the 
    status of the facility after the removal of irradiated fuel from the 
    site.
        Therefore, the proposed changes will not reduce the margins of 
    safety for the remaining plant systems and components.
        The NRC staff has reviewed the licensee's analysis and based on 
    this review the three standards of 50.92(c) are satisfied. The NRC 
    staff agrees with the licensee's analysis and has determined that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Shoreham Wading River Public 
    Library, Shoreham Wading River High School, Route 25A, Shoreham, NY 
    11792
        Attorney for licensee: Mr. W. Taylor Reveley, III, Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 East Byrd Street, Richmond 
    VA 23219-4074
        NRC Branch Chief: John H. Austin
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: February 14, 1994
        Description of amendment requests: The proposed amendments would 
    revise Technical Specifications to reflect the new configuration for 
    the Unit 1 480V safeguards bus arrangement (two 480V safeguards buses 
    fed by each 4160V safeguards bus). This would make the specifications 
    the same for both units since the configuration for the two units will 
    become the same during the outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        SBO/ESU [Station Blackout/Electrical Safeguards Upgrade] Project 
    modifications as reflected in the proposed Technical Specifications 
    changes were evaluated to determine their impact, if any, on 
    potential transients and accidents as described in the Prairie 
    Island USAR [Updated Safety Analysis Report]. Each transient and 
    accident was evaluated in terms of the mitigating actions described 
    or assumed in the USAR analysis. The role of the modified systems in 
    mitigating the event was analyzed in order to evaluate whether the 
    modification:
        (1) changed, degraded or prevented actions described or assumed 
    in the USAR analysis;
        (2) altered any assumptions made in evaluating the radiological 
    consequences of the accident;
        (3) played a direct part in mitigating the radiological 
    consequences of the accident; or
        (4) affected any fission product barrier.
        The evaluation demonstrated that the USAR transient and accident 
    analyses remain valid and bounding.
        As part of the evaluation, the revised emergency diesel 
    generator load sequence was analyzed and found to be bounded by the 
    existing analyses.
        In particular, the USAR analyses of the loss of offsite power 
    (LOOP) event and the large break loss of coolant accident (LBLOCA) 
    remain valid and bounding. In addition, the current USAR analysis 
    for the radiological consequences of a LBLOCA remains valid.
        Further, the plant response to a loss of AC power event is not 
    degraded as a result of these changes but, in fact, is significantly 
    improved.
        In order to determine the effect of the modifications upon the 
    probability and consequences of an accident, the following items 
    were specifically evaluated:
        (1) the applicable design, material and construction standards;
        (2) instrumentation accuracies and response times;
        (3) the equipment operating and design limits, including 
    electrical bus loading, emergency diesel generator loading and 
    battery loading;
        (4) the system interfaces;
        (5) voltage margins; and
        (6) coordination of protective devices.
        Structures, systems and components involved in the modifications 
    were evaluated as follows:
        (1) The design specifications for the new structures, systems 
    and components were considered for the following requirements:
        - seismic;
        - separation including control/power circuit interaction, 
    redundancy/separation of systems, and isolation between safety and 
    non-safety circuits;
        - environmental parameters;
        - severe meteorological events;
        - missiles; and
        - fire protection.
        All structures, systems and components meet the appropriate 
    design requirements for their respective classifications.
        (2) Structures, systems and components were additionally 
    evaluated for the following:
        - Structural loads were determined for new cable runs in the 
    existing plant and for new cable penetrations in the existing 
    structures.
        - New electrical loads requirements were determined.
        - System/equipment protection features have been maintained in 
    the modification.
        - Support system performance was specified to maintain the 
    safety function of the equipment.
        - System/equipment redundancy and independence is maintained.
        - The frequency of operation of existing equipment was evaluated 
    and determined not to be affected.
        - The testing requirements imposed on new structures, systems 
    and components are in accordance with their safety classification.
        Failures of systems and components involved in the modifications 
    were analyzed, and it was determined that all safety functions were 
    maintained.
        Required engineered safeguards features loads are accommodated 
    with the improved auxiliary electrical systems configuration; and, 
    as demonstrated by the performance of a failure modes and affects 
    analysis, no single failure will prevent the modified plant from 
    performing its required safety function in the event of an accident 
    on either unit.
        For the reasons discussed above, the proposed amendment does not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The SBO/ESU Project modifications as reflected in the proposed 
    Technical Specifications changes were evaluated to determine if they 
    could create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The modifications were evaluated to determine the types of 
    accidents which could result from malfunction of the new/modified 
    structures, systems and components. It was determined that no new or 
    different kinds of accidents from those previously evaluated are 
    created. USAR analyses remain bounding.
        For these reasons, the proposed amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The new Unit 1 480V safeguards configuration provides additional 
    circuit breakers for improved motor control center (MCC) feeder 
    circuit coordination by eliminating subfed 480V MCCs from safeguards 
    480V buses. The proposed Technical Specification changes identify 
    the new 480V buses and require the operability of both of the buses 
    per train rather than the one bus per train of the current 
    configuration and current Technical Specification requirements.
        Since the operability requirements are not decreased nor are the 
    allowed out-of-service times increased by the proposed changes, the 
    margin of safety is maintained.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Ledyard B. Marsh
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: February 16, 1994 (Reference LAR 94-03)
        Description of amendment request: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant Unit Nos. 1 and 2 to revise TS 4.6.1.2, ``Containment 
    Integrity.'' The specific TS changes proposed are as follows:
        (1) The requirement to conduct three Type A tests specifically at 
    40 plus or minus 10 month intervals during each 10-year service period 
    would be replaced with a requirement to conduct three Type A tests at 
    approximately equal intervals during each 10-year service period.
        (2) The requirement to conduct the third Type A test of each set 
    during the shutdown for the 10-year plant inservice inspection would be 
    deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes do not affect the initiation of any 
    accident, nor do the proposed changes involve modifications to any 
    plant equipment.
        The proposed change to the schedule provides flexibility in 
    meeting the current requirement for 3 tests in 10 years and is 
    consistent with the intent of the 10 CFR 50, Appendix J requirement 
    to perform Type A tests at approximately equal intervals. The test 
    type and test method used for Type A testing would not be changed. 
    The Type A test acceptance criteria would not be changed, and 
    containment leakage will continue to be maintained within the 
    required limits.
        Elimination of the requirement to perform the third Type A test 
    during the shutdown for the 10-year plant ISI does not involve any 
    modification to plant equipment or affect the operation or design 
    basis of the containment. These surveillances are independent of 
    each other and provide assurance of different plant characteristics. 
    The Type A tests assure the required leak-tightness of the 
    containment to demonstrate compliance with the guidelines of 10 CFR 
    100. The 10-year ISI program provides assurance of the integrity of 
    plant structures, systems, and components and verifies the 
    operational readiness of pumps and valves in accordance with 10 CFR 
    50.55a.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not involve modifications to any 
    existing equipment or affect the operation or design basis of the 
    containment. The proposed changes do not affect the response of the 
    containment during a design basis accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        c. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes to the schedule provide flexibility in 
    meeting the Type A testing schedule requirements. These proposed 
    changes do not affect or change any limiting conditions for 
    operation (LCO) or any other surveillance requirements in the TS and 
    the Bases for the surveillance requirement remains unchanged. The 
    testing method, acceptance criteria, and bases are not changed and 
    still provide assurance that the containment will perform its 
    intended function.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Theodore R. Quay
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: January 10, 1994
        Description of amendment request: The proposed amendment would 
    relocate the seismic monitoring instrumentation Limiting Condition for 
    Operation, Surveillance Requirements, and associated tables and Bases 
    contained in TS sections 3.3.7.2 and 4.3.7.2 to the Updated Final 
    Safety Analysis Report (UFSAR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The function of the seismic monitoring instrumentation system is 
    to monitor the magnitude and effect of a seismic event only, and 
    cannot initiate or mitigate an accident previously evaluated. 
    Furthermore, the proposed TS changes to relocate the seismic 
    monitoring instrumentation requirements from TS to the UFSAR are in 
    accordance with the criteria for determining those requirements that 
    should remain in the TS as defined by the NRC in its final policy 
    statement, ``Final Policy Statement on Technical Specifications 
    Improvements for Nuclear Power Reactors,'' dated July 22, 1993. The 
    seismic monitoring instrumentation LCO, SRs, and associated tables 
    and Bases proposed for relocation from TS to the LGS UFSAR will 
    continue to be implemented by administrative controls that will 
    satisfy the applicable requirements of TS section 6 ``Administrative 
    Controls.'' Those requirements include a review of changes to plant 
    systems and equipment and to the applicable administrative controls 
    in accordance with the provisions of 10CFR50.59.
        Criterion 2 of the July 22, 1993 NRC final policy statement 
    states, ``A process variable, design feature, or operating 
    restriction that is an initial condition of a Design Basis Accident 
    or Transient analysis that either assumes the failure of or presents 
    a challenge to the integrity of a fission product barrier.'' The 
    seismic monitoring instrumentation system is not a system that 
    monitors a process variable that is an initial condition for 
    accident or transient analyses. The seismic monitoring 
    instrumentation is also not a design feature or an operating 
    restriction that is an initial condition of Design Basis Accident or 
    transient analyses since it only provides information regarding the 
    magnitude of and the plant equipment response to a Design Basis 
    earthquake. Therefore, the current LGS seismic monitoring 
    instrumentation TS requirements do not meet Criterion 2 of the July 
    22, 1993 NRC final policy statement.
        Criterion 3 of the July 22, 1993 NRC final policy statement 
    states, ``A structure, system, or component that is part of the 
    primary success path and which functions or actuates to mitigate a 
    Design Basis Accident or Transient that either assumes the failure 
    of or presents a challenge to the integrity of a fission product 
    barrier.'' The LGS seismic monitoring instrumentation system does 
    not provide a function or actuate in order to mitigate the 
    consequences of a Design Basis Accident or transient. Therefore, the 
    current LGS seismic monitoring instrumentation TS requirements do 
    not meet Criterion 3 of the July 22, 1993 NRC final policy 
    statement.
        Criterion 4 of the July 22, 1993 NRC final policy statement 
    states, ``A structure, system or component which operating 
    experience or probabilistic safety assessment has shown to be 
    significant to public health and safety.'' Operating experience has 
    shown that the LGS seismic monitoring instrumentation system has no 
    impact on public health and safety as defined by the NRC final 
    policy statement. Furthermore, LGS specific probabilistic risk 
    assessment (PRA) does not credit the seismic monitoring 
    instrumentation system as a significant factor in the plant response 
    to an accident. Therefore, the current LGS seismic monitoring 
    instrumentation TS requirements do not meet Criterion 4 of the July 
    22, 1993 NRC final policy statement for determining those 
    requirements that should remain in TS. This conclusion is consistent 
    with the function of the seismic monitoring instrumentation system 
    stated above.
        These proposed TS changes will maintain the current operation, 
    maintenance, testing, and system operability controls of the seismic 
    monitoring instrumentation system. Furthermore, any future changes 
    to the seismic monitoring instrumentation system will be evaluated 
    for the effect of those changes on system reliability as required by 
    10CFR50.59. The seismic monitoring instrumentation system 
    performance will not decrease due to these proposed TS changes and 
    the system will continue to be administratively controlled in 
    accordance with TS Section 6, including the requirements of 
    10CFR50.59, thereby precluding a future decrease in its performance.
        In accordance with the current TS Section 3.3.7.2, with the 
    seismic monitoring instrumentation inoperable, the plant would not 
    be required to shutdown and the provisions of TS Section 3.0.3 
    (i.e., plant shutdown) would not be applicable. Therefore, the 
    inoperability of this system and therefore the consequences of an 
    accident while this system is inoperable, was previously evaluated 
    as not significant enough to require a change to the plant operating 
    condition.
        Since the seismic monitoring instrumentation system does not 
    monitor a process variable that is an initial condition for an 
    accident or transient analyses, or actuates any accident mitigation 
    feature, and since the operation, maintenance, testing, and 
    modification of the seismic monitoring instrumentation system will 
    continue to be administratively controlled, including the 
    requirements of 10CFR50.59; therefore, maintaining the reliability 
    of the system, the proposed TS changes will not involve an increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The function of the seismic monitoring instrumentation system is 
    to monitor the magnitude and effect of a seismic event only. The 
    proposed TS changes to relocate the seismic monitoring instruments 
    requirements from TS to the UFSAR are in accordance with the 
    criteria for determining those requirements that should remain in 
    the TS as defined by the NRC in its final policy statement, dated 
    July 22, 1993. The seismic monitoring instrumentation system does 
    not monitor a process variable that is an initial condition for an 
    accident or transient analyses. The seismic monitoring 
    instrumentation is also not a design feature or an operating 
    restriction that is an initial condition of a Design Basis Accident 
    or transient analyses since it only provides information regarding 
    the magnitude of and the plant equipment response to a Design Basis 
    earthquake.
        These proposed TS changes to relocate the TS requirements to the 
    UFSAR will not alter the operation of the plant, or the manner in 
    which the seismic monitoring instrumentation system will perform its 
    function, and any future changes will continue to be 
    administratively controlled in accordance with TS Section 6, 
    including the requirements of 10CFR50.59.
        These proposed TS changes will not impose new conditions nor 
    result in new types of equipment which will result in different 
    types of malfunctions of equipment important to safety than any type 
    previously evaluated.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        These proposed TS changes to relocate the seismic monitoring 
    instrumentation requirements from TS to the UFSAR are in accordance 
    with the criteria for determining those requirements that should 
    remain in the TS as defined by the NRC in final policy statement, 
    dated July 22, 1993.
        Criterion 1 of the NRC final policy statement states, 
    ``Installed instrumentation that is used to detect, and indicate in 
    the control room, a significant abnormal degradation of the reactor 
    coolant pressure boundary.'' The NRC final policy statement explains 
    that ''...This criterion is intended to ensure that Technical 
    Specifications control those instruments specifically installed to 
    detect excessive reactor coolant leakage. This criterion should not, 
    however, be interpreted to include instrumentation to detect 
    precursors to reactor coolant pressure boundary leakage or 
    instrumentation to identify the source of actual leakage (e.g., 
    loose parts monitor, seismic instrumentation, valve position 
    indicators).'' Based on the above NRC guidance, the LGS UFSAR, and 
    TS Bases 3.3.7.2, the seismic monitoring instrumentation does not 
    detect, and indicate in the control room, a significant abnormal 
    degradation of the reactor coolant pressure boundary. Therefore, the 
    current LGS seismic monitoring instrumentation TS requirements do 
    not meet Criterion 1. Furthermore, operating experience has shown 
    that the LGS seismic instrumentation system has no impact on public 
    health and safety as defined by the NRC final policy statement. In 
    addition, the LGS specific PRA does not credit the seismic 
    monitoring instrumentation system as a significant factor in the 
    plant response to accidents.
        The seismic monitoring instrumentation LCO, SRs, and associated 
    tables and Bases proposed for relocation to the LGS UFSAR will 
    continue to be implemented by administrative controls that will 
    satisfy the applicable requirements of TS section 6 ``Administrative 
    Controls.'' Those requirements include a review of future changes to 
    the system and applicable administrative controls in accordance with 
    the provisions of 10CFR50.59.
        Accordingly, based on the above discussion of NRC specific 
    guidance, operating experience, and continued imposition of 
    administrative controls, the proposed TS changes do not involve a 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Charles L. Miller
    
    Power Authority of The State of New York, Docket No. 50 286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: February 3, 1994
        Description of amendment request: The licensee commenced operating 
    on a 24-month fuel cycle, instead of the previous 18-month fuel cycle, 
    with fuel cycle 9. Fuel cycle 9 started in August 1992; however, the 
    facility shut down in February 1993 for a ``Performance Improvement 
    Plan'' outage and a restart date has not yet been established. In order 
    to accommodate operation on a 24-month cycle after the facility 
    restarts, the licensee requested an amendment to the Technical 
    Specifications (TSs) to incorporate the changes listed in items 1-7 
    below:
        (1) The licensee proposed changing the calibration frequency for 
    the reactor coolant temperature instrument channels (specified in TS 
    Table 4.1-1) to accommodate operation on a 24-month cycle.
        (2) The licensee proposed changing the calibration frequency for 
    the steam generator level instrument channels (specified in TS Table 
    4.1-1) to accommodate operation on a 24-month cycle.
        (3) The licensee proposed changing the calibration frequency for 
    the containment pressure instrument channels (specified in TS Table 
    4.1-1) to accommodate operation on a 24-month cycle.
        (4) The licensee proposed changing the calibration frequency for 
    the steam line pressure instrument channels (specified in TS Table 4.1-
    1) to accommodate operation on a 24-month cycle.
        (5) The licensee proposed changing the calibration frequency for 
    the turbine first stage pressure instrument channels (specified in TS 
    Table 4.1-1) to accommodate operation on a 24-month cycle.
        (6) The licensee proposed changing the calibration frequency for 
    the turbine trip low auto stop oil pressure instrument channels 
    (specified in TS Table 4.1-1) to accommodate operation on a 24-month 
    cycle.
        (7) The licensee proposed changing the calibration frequency for 
    the 480V bus undervoltage and alarm relays (specified in TS Table 4.1-
    1) to accommodate operation on a 24-month cycle.
        These proposed changes follow the guidance provided in Generic 
    Letter 91-04, ``Changes in Technical Specification Surveillance 
    Intervals to Accommodate a 24-Month Fuel Cycle,'' as applicable.
        The licensee also requested the following additional changes:
        (1) The addition to TS Table 3.5-5 of limiting conditions for 
    operation (LCO) requirements for a wide range containment pressure 
    variable.
        (2) The addition of a quarterly functional test surveillance 
    requirement to Item 4 of TS Table 4.1-1 for the low average temperature 
    actuation circuits of the reactor coolant temperature channels.
        (3) The addition of a second line to Item 14 of TS Table 4.1-1 to 
    specify surveillance requirements for the wide range containment 
    pressure instrumentation.
        (4) The revision of Item 20 to TS Table 4.1-1 to clarify that both 
    the reactor trip and the engineered safety features (ESF) actuation 
    relay logic channels are functionally tested.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Consistent with the criteria of 10 CFR 50.92, the enclosed 
    application is judged to involve no signicant hazards based on the 
    following information:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated?
        Response:
        The proposed changes do not involve a significant increase in 
    the probability or consequences of any accident previously 
    evaluated. The proposed changes extend the calibration intervals 
    (given in [TS] Table 4.1-1) for the reactor coolant loop temperature 
    instrumentation used for Engineered Safety Features Actuation 
    Systems (ESFAS) and Post Accident Monitoring (PAM) functions, the 
    steam generator (SG) level instrumentation used for ESFAS and PAM 
    functions, the containment pressure instrumentation used for ESFAS 
    and PAM functions, the steam line pressure instrumentation used for 
    ESFAS and PAM functions, the turbine first stage pressure 
    instrumentation used for ESFAS functions, the 480V bus undervoltage 
    and alarm relays used for ESFAS functions, and the turbine trip low 
    auto stop oil pressure instrumentation. These changes are being made 
    to accommodate a 24 month operating cycle. Other changes include: 1) 
    the addition to [TS] Table 3.5-5 of limiting conditions for 
    operation (LCO) requirements for the wide range containment pressure 
    channels; 2) the addition of a quarterly functional test 
    surveillance requirement to Item 4 of [TS] Table 4.1-1 for the low 
    Tavg [average temperature] actuation circuits of the reactor 
    coolant temperature channels; 3) the addition of a second line to 
    Item 14 of [TS] Table 4.1-1 to specify the surveillance requirements 
    for the wide range containment pressure channels; and 4) the 
    revision of Item 20 to [TS] Table 4.1-1.
        Extension of the calibration intervals in question were 
    evaluated and the results documented in the ESFAS and Indicating 
    Instrument Surveillance Test Extension reports (References 7 and 8 
    [Engineered Safety Features Actuation Systems Surveillance Test 
    Extensions, NYPA document IP3-RPT-ESS-00400, dated May 10, 1993 and 
    Indicating Instruments Surveillance Test Extensions, NYPA document 
    IP3-RPT-MULTI-00424, dated May 5, 1993]). ESFAS and indicating 
    instrument drift analyses were performed to evaluate actual past and 
    projected future instrument drift. Revised safety system loop 
    accuracy/setpoint calculations, which include any additional 
    instrument uncertainties resulting from the proposed calibration 
    interval extensions, show that sufficient margin exists between the 
    analytical and field trip settings for the low Tavg, the SG 
    low-low level, the high and high-high containment pressure, the high 
    differential steam line pressure, the low steam line pressure, the 
    high steam flow (dependent upon turbine first stage pressure), the 
    turbine trip low auto stop oil pressure, and the 480V bus 
    undervoltage trip functions. Safety analyses are not affected. 
    Additionally, postulated uncertainties associated with the extended 
    calibration intervals for the wide range reactor coolant loop 
    temperature, the narrow and wide range SG level, and the steam line 
    pressure instrumentation will be accomodated by changes to the 
    Emergency Operating Procedure (EOP) settings. Extension of the 
    calibration interval for the narrow range containment pressure 
    instrumentation channels does not affect EOP settings. Safety 
    analyses are not affected by the EOP setting changes.
        The results of the changes to: 1) add to [TS] Table 3.5-5 LCO 
    requirements for the wide range containment pressure channels, 2) 
    add a quarterly functional test surveillance requirement to Item 4 
    of [TS] Table 4.1-1 for the low Tavg actuation circuits of the 
    reactor coolant temperature channels, and 3) add a monthly channel 
    check surveillance requirement to [TS] Table 4.1-1 for the wide 
    range containment pressure channels are consistent with Westinghouse 
    Standard Technical Specifications (W STS - Reference 12 [NUREG-1431, 
    Revision O, ``Standard Technical Specifications - Westinghouse 
    Plant,'' dated September 28, 1992]). The addition of LCO 
    requirements to [TS] Table 3.5-5 for the wide range containment 
    pressure instrumentation, the addition of a quarterly functional 
    test requirement to Item 4 of [TS] Table 4.1-1 for the low Tavg 
    actuation circuits, and the separation of surveillance requirements 
    for the narrow and wide range containment pressure instrumentation 
    into two lines on [TS] Table 4.1-1 consitute additional technical 
    specification controls. Changes which consitute additional technical 
    specification limitations and controls are classified by Federal 
    Register dated April 6, 1983 (48 FR 14870, April 6, 1983) as not 
    likely to involve significant hazards considerations. The change to 
    [TS] Table 3.5-5 ensures conistency with the Authority's commitment 
    to Regulatory Guide (RG) 1.97 [``Instrumentation for Light-Water-
    Cooled Nuclear Power Plants to Assess Plant and Environs Conditions 
    During and Following an Accident''] for the containment pressure 
    variable.
        The current surveillance requirement specified by Item 20 has 
    been interpreted by Indian Point 3 as including on-line testing of 
    both the reactor trip and engineered safety features (ESF) actuation 
    logic channels, but since the wording may be confusing, this 
    application proposes to change the wording to clarify that both the 
    reactor trip and the ESF actuation logic channels are functionally 
    tested at least every two months on a staggered basis (i.e., one 
    train per month). The change is consistent with W STS and only 
    involves a wording change which strengthens the Technical 
    Specification requirement. The change does not involve hardware, 
    procedural, or operational changes, and, therefore, does not affect 
    safety analyses.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any previously 
    evaluated?
        Response:
        The proposed changes do not create the possibility of a new or 
    different kind of accident from any previously evaluated. Extension 
    of the calibration intervals in question were evaluated and the 
    results documented in the ESFAS and Indication Instrument 
    Surveillance Test Extension reports. ESFAS and indicating instrument 
    drift analyses were performed to evaluate actual past and projected 
    future instrument drift. Revised safety system loop accuracy/
    setpoint calculations and EOP setting calculations show that, 
    although some EOP setting changes will be made to accommodate 
    postulated drift associated with the extended calibration intervals, 
    safety analyses are not affected.
        The changes to 1) specify LCO and surveillance requirements for 
    the wide range containment pressure instrumentation channels, 2) add 
    a quarterly functional test surveillance requirement to Item 4 of 
    [TS] Table 4.1-1 for the low Tavg actuation circuits of the 
    reactor coolant temperature channels, and 3) clarify that both 
    reactor trip and ESF actuation logic channels are functionally 
    tested constitute additional technical specification limitation and 
    controls. Additionally, these changes are consistent with W STS.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        The proposed changes do not involve significant reductions in 
    margins of safety. Loop accuracy/setpoint calculations show that 
    sufficient margin exists between the analytical and field trip 
    settings for the low Tavg, the SG low-low level, the high and 
    high-high containment pressure, the high differential steam line 
    pressure, the low steam line pressure, the high steam flow 
    (dependent upon turbine first stage pressure), the turbine trip low 
    auto stop oil pressure, and the 480V bus undervoltage trip functions 
    to accommodate postulated uncertainties associated with the extended 
    calibration intervals. And, although changes to EOP settings will be 
    made to accommodate the postulated uncertainties associated with the 
    extended calibration intervals for the wide range reactor coolant 
    loop temperature, the narrow and wide range SG level, and the steam 
    line pressure instrumentation, the EOP setting changes do not in any 
    way adversely affect the analytical limits established by safety 
    analyses.
        Extension of the calibration intervals in question do not affect 
    safety analyses. The other changes being made in this application 
    involve additional technical specification limitations and controls 
    and are consistent with W STS. None of the changes involve 
    significant reductions in margins of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: Robert A. Capra
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: March 4, 1994
        Description of amendment request: The proposed change would modify 
    Sections 5.3 and 5.6 of the Technical Specifications (TSs) to allow the 
    use of Westinghouse Vantage+ fuel with ZIRLO cladding. The present TSs 
    require the fuel rod cladding to be Zircaloy-4, which is used in the 
    Westinghouse Standard and Vantage 5H fuel designs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes to Technical Specifications 5.3.1 and 5.6.1 
    for Salem Generating Station (SGS) Unit Nos. 1 and 2:
        1. do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The fuel cladding design criteria for SGS would remain the same 
    for ZIRLO clad fuel as it is for Zircaloy-4 clad fuel. All fuel 
    design and performance criteria will continue to be met using NRC-
    approved methods and no new single failure mechanisms will be 
    introduced. The use of ZIRLO clad fuel does not introduce any 
    changes to plant equipment or operation that would adversely affect 
    accident initiators or precursors. The proposed changes would not 
    result in any changes to compliance with licensing basis safety 
    limits.
        2. do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed changes would require that NRC[-]approved methods 
    be used in fuel assembly design. No new operating configurations 
    potentially resulting in the occurrence of a previously unanalyzed 
    event would be allowed by the proposed change.
        3. do not involve a significant reduction in a margin of safety.
        The proposed change would continue to require that NRC[-
    ]approved methods are used to ensure compliance with the fuel design 
    and safety limits which ensure that an acceptable margin of safety 
    is maintained relative to fuel assembly design.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: Charles L. Miller
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: March 1, 1993
        Description of amendment request: The proposed amendment would 
    clarify Technical Specification 3.6.1.2, Primary Containment Leakage, 
    and revise the ``as-found'' value of the overall integrated primary 
    containment leakage rate which is used when determining the test 
    schedule for future Type A tests within Surveillance Requirement 
    4.6.1.2.b. This amendment also requests an exemption from the 
    requirements of 10 CFR 50 Appendix J, Primary Reactor Containment 
    Leakage Testing for Water-Cooled Power Reactors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        These proposed changes clarify Technical Specification 3.6.1.2 
    by providing a more definitive action to take if the leakage rate 
    limit(s) specified in the LCO are not being met. The current Action 
    is not clear on what actions are necessary if the leakage rate 
    limits (e.g., Type B and C limits) are known to be exceeded while 
    the reactor coolant system (RCS) temperature is above 200 deg. F, 
    which has caused compliance difficulties. The revised Action is 
    modeled after the one in the Primary Containment Integrity 
    Specification, which (through the definition of Primary Containment 
    Integrity) includes a provision that the containment leakage rates 
    be in compliance with the requirements of Specification 3.6.1.2.
        Surveillance Requirement 4.6.1.2.b has been revised to reflect 
    the actual plant design basis leakage rate of La as the value 
    against which the ``as-found'' Type A test results are compared when 
    determining the test schedule for future Type A tests. The 
    probability of exceeding the maximum allowable leakage rate, 
    La, is not significantly increased since the ``as-left'' 
    leakage rate requirement of 0.75 La (which must be met during 
    startup from any outage in which a Type A test has been performed) 
    is still imposed through LCO 3.6.1.2.a, Action 3.6.1.2.a and 
    Surveillance Requirement 4.6.1.2.a. The Applicability of 
    Specification 3.6.1.2 has been modified to resolve an existing 
    conflict with the current Action, which requires that a reactor 
    coolant system temperature of 200 deg. F not be exceeded with a 
    leakage rate greater than 0.75 La (during startups from outages 
    in which a Type A ILRT has been performed). With the modified 
    Applicability and the retained LCO requirement for the ``as-left'' 
    leakage rate to be less than or equal to 0.75 La, the 
    requirement of the current Action (not to exceed to 200 deg. F) is 
    implicitly maintained, due to the provisions contained within 
    specification 3.0.4. This maintains the same margin for degradation 
    between performances of the periodic Type A tests as is provided in 
    the current specification. Since the analysis leakage limit of 
    La has not changed, the offsite radiological consequences of an 
    accident assumed in the safety analyses have not been affected.
        The deletion of the current link between Specifications 3.6.1.2 
    and 3.10.1 is an administrative change only, made because the two 
    Specifications no longer overlap and the link is therefore 
    unnecessary.
        In summary, there is no change in the probability or 
    consequences of any accident since the clarifications of the 
    existing LCO, Applicability, Actions, Surveillance Requirements and 
    the revised ``as-found'' acceptance criterion do not change the 
    design of the plant, nor the operational characteristics of any 
    plant system, nor the procedures by which the Operators run the 
    plant.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed Action to address situations when the leakage rate 
    limit(s) cannot be met in Operational Conditions 1, 2 and 3, with 
    the reactor coolant system temperature greater than 200 deg. F, does 
    not create the possibility of a new or different kind of event - it 
    only provides the measures to be taken following determination of 
    increased containment leakage. The clarification to the existing 
    Applicability simply resolves an existing conflict between the 
    Applicability and the Action, and ensures that the same requirements 
    that were contained within the former Action are maintained 
    following implementation of the change, by preventing plant startup 
    above a RCS temperature of 200 deg. F (following an outage in which 
    a Type A test has been performed), unless the leakage rate is below 
    the 0.75 La test acceptance criterion. Additional changes are 
    being made to clarify the application of Appendix J requirements.
        Revising the ``as-found'' value of La does not create the 
    possibility of a new or different kind of event - since the analysis 
    limit value, La, has not been increased and no new mode of 
    operation has been introduced.
        In summary, the proposed changes do not create the possibility 
    of a new or different kind of accident, since no design changes are 
    being made that would create a new type of accident or malfunction, 
    and the method and manner of plant operation remains unchanged.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed Action simply imposes a more definitive action to 
    take when a leakage rate limit(s) is exceeded, consistent with the 
    Primary Containment Integrity Specification. The changes to the 
    Surveillance Requirements to reflect the ``as-found'' value of 
    La are consistent with the intent of the requirements specified 
    in Appendix J, and similar requirements have been provided for other 
    plants. The current requirement for ``as-left'' leakage rates to be 
    less than or equal to 0.75 La before increasing the reactor 
    coolant system temperature above 200 deg. F from outages in which a 
    Type A ILRT has been performed has been retained since the proposed 
    Action now includes a shutdown requirement, and in accordance with 
    Technical Specification 3.0.4, ``Entry into an OPERATIONAL CONDITION 
    or other specified condition shall not be made when the conditions 
    for the LCO are not met and the associated ACTION requires a 
    shutdown if they are not met within a specified time interval.'' 
    Since the new Action includes a shutdown provision and the LCO 
    retains the current limit of 0.75 La, a change into the new 
    Applicability of Specification 3.6.1.2 cannot occur if 0.75 La 
    is exceeded. This ensures that the same margin as currently exists 
    today is maintained for possible degradation between performance of 
    the periodic Type A tests. The other changes are clarifications and 
    are administrative in nature. Therefore, the proposed changes do not 
    involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, D.C. 20037
        NRC Project Director: John N. Hannon
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: February 10, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Table 2.2-1 and Bases Section 2.2.1. The 
    Functional Unit 14 of Table 2.2-1 would be revised to correct the Total 
    Allowance, reflecting the undervoltage relay span and to correct the 
    Allowable Value, reflecting the rack measurement and test equipment 
    (M&TE) uncertainty. The Bases would be revised to clarify the 
    relationship between the Trip Setpoint and Allowable Value, expressed 
    in voltage, and the Total Allowance, Z and S values, expressed in 
    percent of the undervoltage relay span (calibrated span of 70-100 
    volts).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve a significant hazards 
    consideration because operation of the Callaway Plant with these 
    changes would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Overall protection system performance will remain within the 
    bounds of the accident analyses documented in FSAR Chapter 15, WCAP-
    10961-P, and WCAP-11883 since no hardware changes are proposed.
        The RCP undervoltage reactor trip function is a primary trip 
    function and is credited in FSAR Section 15.3.2, Complete Loss of 
    Forced Reactor Coolant Flow. The trip setpoint is designed to ensure 
    plant operation within the DNB design basis. There will be no effect 
    on this analysis, or any other accident since the safety analysis 
    limit and trip response time are unaffected and remain the same as 
    discussed in FSAR Section 15.0.6 and FSAR Table 15.0.4.
        The RCP undervoltage reactor trip will continue to function in a 
    manner consistent with the above analysis assumptions and the plant 
    design basis. As such, there will be no degradation in the 
    performance of nor an increase in the number of challenges to 
    equipment assumed to function during an accident situation.
        These Technical Specification revisions do not involve any 
    hardware changes nor do they affect the probability of any event 
    initiators. There will be no change to normal plant operating 
    parameters, ESF actuation setpoints, accident mitigation 
    capabilities, accident analysis assumptions or inputs. Therefore, 
    these changes will not increase the probability of an accident 
    previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any previously evaluated.
        As discussed above, there are no hardware changes associated 
    with these Technical Specification revisions nor are there any 
    changes in the method by which any safety-related plant system 
    performs its safety function.
        Changes to the Total Allowance and Allowable Value terms in 
    Technical Specification Table 2.2-1 will require only minor changes 
    to the acceptance criteria sections of a few surveillance 
    procedures. The normal manner of plant operation is unaffected. If 
    an undervoltage relay setpoint is found to be below the nominal trip 
    setpoint in Table 2.2-1, entry into Action Statements a or b of 
    Specification 2.2.1 will be affected insofar as the Allowable Value 
    is being lowered and the Total Allowance value contained in Equation 
    2.2-1 is being raised. However, the nominal trip setpoint is 
    unchanged and the required plant condition for exiting the Action 
    Statements, i.e. adjusting the trip setpoint consistent with the 
    Table 2.2-1 value, is likewise unchanged. The revisions to the Total 
    Allowance and Allowable Value correct errors in their derivation and 
    were calculated using the previously approved Westinghouse setpoint 
    methodology. The setpoint equations cited in that methodology are 
    unchanged; however, inputs to those equations have been revised to 
    reflect the undervoltage relay span and the rack M&TE uncertainty.
        No new accident scenarios, transient precursors, failure 
    mechanism, or limiting single failures are introduced as a result of 
    these changes. There will be no adverse effect or challenges imposed 
    on any safety-related system as a result of these changes. 
    Therefore, the possibility of a new or different type of accident is 
    not created.
        (3) Involve a significant reduction in a margin of safety.
        There will be no change to the DNBR Correlation Limit, the 
    design DNBR limits, or the safety analysis DNBR limits discussed in 
    Bases Section 2.1.1.
        As discussed previously, the response time of the RCP 
    undervoltage reactor trip function will remain within the 
    assumptions used in the accident analyses. The analysis of the 
    complete loss of flow accident will remain as presented in FSAR 
    Section 15.3.2.
        There will be no effect on the manner in which safety limits or 
    limiting safety system settings are determined nor will there be any 
    effect on those plant systems necessary to assure the accomplishment 
    of protection functions. There will be no impact on DNBR limits, 
    FQ, F-delta-H, LOCA PCT, peak local power density, or any other 
    margin of safety. The safety analysis limit, 9384 Vac at the RCP 
    motor, and the nominal trip setpoint, 10,584 Vac, remain the same as 
    before.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: John N. Hannon
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of amendment request: February 17, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications 3/4.5.1 and Bases Section 3/4.5.1. A 
    new Action Statement a. would be added to Specification 3.5.1 to 
    provide a 72 hour allowed outage time (AOT) for one accumulator 
    inoperable due to its boron concentration not meeting the 2300-2500 ppm 
    band. The AOT for Action Statement b. would be changed to 24 hours in 
    lieu of the current AOT of 1 hour. Surveillances 4.5.1.1.a.1) and 
    4.5.1.1.b would be revised and Surveillance 4.5.1.2 would be deleted 
    per the guidance of NRC Generic Letter 93-05. Bases Section 3/4.5.1 
    would be revised to discuss the 72 hour and 24 hour AOTs for Action 
    Statements a. and b. above.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes to the Technical Specifications do not 
    involve a significant hazards consideration because operation of 
    Callaway Plant in accordance with these changes would not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Overall protection system performance will remain within the 
    bounds of the accident analyses documented in FSAR Chapter 15, WCAP-
    10961-P, and WCAP-11883 since no hardware changes are proposed.
        The safety injection (SI) accumulators are credited in FSAR 
    Section 15.6.5 for large and small break LOCA. There will be no 
    effect on these analyses, or any other accident analysis, since the 
    analysis assumptions are unaffected and remain the same as discussed 
    in FSAR Section 15.6.5. Design basis accidents are not assumed to 
    occur during allowed outage times covered by the Technical 
    Specifications. As such, the ECCS Evaluation Model equipment 
    availability assumptions made in FSAR Section 15.6.5 remain valid.
        The SI accumulators will continue to function in a manner 
    consistent with the above analysis assumptions and the plant design 
    basis. As such, there will be no degradation in the performance of 
    nor an increase in the number of challenges to equipment assumed to 
    function during an accident situation.
        These Technical Specification revisions do not involve any 
    hardware changes nor do they affect the probability of any event 
    initiators. There will be no change to normal plant operating 
    parameters, ESF actuation setpoints, accident mitigation 
    capabilities, accident analysis assumptions or inputs. The effect on 
    the Callaway core damage frequency has been quantified as 
    insignificant. Therefore, these changes will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any previously evaluated.
        As discussed above, there are no hardware changes associated 
    with these Technical Specification revisions nor are there any 
    changes in the method by which any safety-related plant system 
    performs its safety function. The normal manner of plant operation 
    is unaffected.
        No new accident scenarios, transient precursors, failure 
    mechanisms, or limiting single failures are introduced as a result 
    of these changes. There will be no adverse effect or challenges 
    imposed on any safety-related system as a result of these changes. 
    Therefore, the possibility of a new or different type of accident is 
    not created.
        (3) Involve a significant reduction in a margin of safety.
        There will be no change to the DNBR Correlation Limit, the 
    design DNBR limits, or the safety analysis DNBR limits discussed in 
    Bases Section 2.1.1.
        As discussed previously, the performance of the SI accumulators 
    will remain within the assumptions used in the large and small break 
    LOCA analyses, as presented in FSAR Section 15.6.5.
        There will be no effect on the manner in which safety limits or 
    limiting safety system settings are determined nor will there be any 
    effect on those plant systems necessary to assure the accomplishment 
    of protection functions. There will be no impact on DNBR limits, 
    FQ, F-delta-H, LOCA PCT, peak local power density, or any other 
    margin of safety.
        Based upon the preceding information, it has been determined 
    that the proposed changes to the Technical Specifications do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated, create the possibility of a new or 
    different kind of accident from any accident previously evaluated, 
    or involve a significant reduction in a margin of safety. Therefore, 
    it is concluded that the proposed changes meet the requirements of 
    10CFR50.92(c) and do not involve a significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, DC 20037.
        NRC Project Director: John N. Hannon
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: March 1, 1994
        Description of amendment request: The proposed change would revise 
    the Technical Specifications (TS) for the North Anna Power Station, 
    Units No. 1 and No. 2 (NA-1&2). Specifically, the change would 
    eliminate certain surveillance requirements for the emergency diesel 
    generators which have been determined to be unnecessary.
        The NRC has completed a comprehensive examination of surveillance 
    requirements in TS that require testing at power. The evaluation is 
    documented in NUREG-1366, ``Improvements to Technical Specification 
    Surveillance Requirements,'' dated December 1992. The NRC staff found, 
    that while the majority of testing at power is important, safety can be 
    improved, equipment degradation decreased, and an unnecessary burden on 
    personnel resources eliminated by reducing the amount of testing at 
    power that is required by TS. Based on the results of the evaluations 
    documented in NUREG-1366, the NRC issued Generic Letter 93-05, ``Line-
    Item Technical Specifications Improvements to Reduce Surveillance 
    Requirements for Testing During Power Operation,'' dated September 27, 
    1993.
        The safety function of the Emergency Diesel Generators (EDGs) is to 
    supply AC electrical power to plant safety systems whenever the 
    preferred AC power supply is unavailable. Consistent with Generic 
    Letter 93-05, Item 10.1 and NUREG-1366, the licensee is requesting a 
    change to the testing requirements of an operable EDG when the 
    alternate safety buses' EDG is inoperable or an offsite circuit is 
    inoperable, the separation of the hot restart test of an EDG from the 
    24 hour loaded run, and the elimination of fast loading of EDGs except 
    for the 18 month surveillance test of the Loss of Offsite Power (LOOP) 
    capability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of North Anna Power Station in 
    accordance with the proposed Technical Specifications changes will 
    not:
        (1) Involve a significant increase in the probability of 
    occurrence or consequences of an accident previously evaluated.
        Modifying the operability testing requirements for an inoperable 
    EDG or inoperable offsite AC source(s), gradual loading of EDGs 
    during surveillance testing, and separating the hot restart test of 
    an EDG from the 24 hour load run test of EDGs does not affect the 
    probability of occurrence or consequences of any previously 
    evaluated accidents. Surveillance testing of the EDG in accordance 
    with Revision 2 of Regulatory Guide 1.9 (December 1979) will 
    continue to ensure that the EDGs will be capable of performing their 
    intended safety functions. Therefore, modifying the operability 
    testing requirements for an inoperable EDG or inoperable offsite AC 
    source(s), gradual loading of EDGs during surveillance testing, and 
    separating the hot restart test of an EDG from the 24 hour load run 
    test of EDGs does not affect the probability or consequences of any 
    previously analyzed accident.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Modifying the operability testing requirements for an inoperable 
    EDG or inoperable offsite AC source(s), gradual loading of EDGs 
    during surveillance testing, and separating the hot restart test of 
    an EDG from the 24 hours load run test of EDGs does not involve any 
    physical modifications of the plant or result in a change in a 
    method of operation. Surveillance testing of the EDG in accordance 
    with Revision 2 of Regulatory Guide 1.9 (December 1979) will 
    continue to ensure that the EDGs will be capable of performing their 
    intended safety functions. Therefore, a new or different type of 
    accident is not made possible.
        (3) Involve a significant reduction in a margin of safety.
        Modifying the operability testing requirements for an inoperable 
    EDG or inoperable offsite AC source(s), gradual loading of EDGs 
    during surveillance testing, and separating the hot restart test of 
    an EDG from the 24 hour load run test of EDGs does not affect any 
    safety limits or limiting safety systems settings. System operating 
    parameters are unaffected. The availability of equipment required to 
    mitigate or assess the consequences of an accident is not reduced. 
    Surveillance testing of the EDG in accordance with Revision 2 of 
    Regulatory Guide 1.9 (December 1979) will continue to assure that 
    the EDGs will be capable of performing their intended safety 
    functions. Safety margins are, therefore, not decreased.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Herbert N. Berkow
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: May 10, 1993
        Description of amendment request: The amendment proposes to modify 
    the Technical Specifications (TS) to incorporate new power to flow 
    limits based on core power stability calculations performed for Cycle 
    9. In addition, the proposed amendment would clarify the maximum 
    measured decay ration permitted during operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's evaluation of 
    the licensee's analysis is presented below:
        1. Does the amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change related to the instability regions on the power 
    to flow map is based on new calculations using a new code (STAIF) while 
    maintaining a decay ration of 0.9 or less as required in IEB 88-07. The 
    closer the operators come to a decay ration of 1.0, the closer the core 
    comes to potential core power instabilities. By ensuring that the decay 
    ratio is maintained below 0.9, the operators reduce the likelihood of 
    core power instabilities. The result of the revised calculations using 
    this new code is that the restricted regions are expanded over the 
    regions contained in the current TS. This increase in restricted 
    regions results in plant operation further from potential core power 
    instabilities compared to the restricted regions in the current TS, 
    resulting in a decreased probability of core power oscillations. The 
    power to flow map regions are operating restrictions that, for the core 
    power oscillation restricted regions, are intended to reduce the 
    likelihood of the onset of oscillations. The core power oscillation 
    restricted regions on the power to flow map do not contribute to any 
    mitigative actions or plant response after a power oscillation occurs, 
    thus the proposed change does not change the consequences of any 
    accidents previously evaluated.
        The proposed amendment would also change the wording of the 
    technical specifications to clarify that action must be taken to reduce 
    the measured decay ration if any two neutron signals of ``greater than 
    or equal to 0.75,'' as opposed to the current wording ``greater than 
    .75,'' are measured. This would not have any measurable effect on the 
    implementation of the affected TS, and would, if anything, result in 
    action being taken at a maximum lower value than the current TS. This 
    proposed amendment would not, therefore, involve a change in the 
    probability or consequences of an accident previously evaluated.
        2. Does the amendment create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change; modifies existing restrictions on the power to 
    flow map, and does not involve any modifications to plant systems or 
    components or the manner in which they are operated.
        Changing the wording of the TS to require that action be taken to 
    reduce the measured decay ration if any two neutron signals of 
    ``greater than or equal to 0.75,'' as opposed to the current wording 
    ``greater than .75,'' are measured, does not involve any modifications 
    to plant systems or components or the manner in which they are 
    operated.
        Based on these considerations, this does not create or increase the 
    possibility of a new or different kind of accident.
        3. Does the amendment involve a significant reduction in a margin 
    of safety?
        The margin of safety related to the proposed TS change is the core 
    power vs. core flow restrictions on the power to flow map. These 
    restrictions are currently based on maintaining a decay ratio less than 
    0.9, which provides a margin of at least a decay ration of 0.1 from 
    what is defined as a decay ration (1.0) that would result in an 
    unstable core. Since the revised curves are based on ensuring decay 
    rations of less than 0.9 are maintained, the existing margin of safety 
    is maintained.
        Changing the wording of the TS to require that action be taken to 
    reduce the measured decay ratio if any two neutron signals of ``greater 
    than or equal to 0.75,'' as opposed to the current wording ``greater 
    than .75,'' are measured, would not have any measurable effect on the 
    implementation of the affected TS, and would, if anything, result in 
    action being taken at a maximum lower value than the current TS. This 
    would not have any significant impact on how close the plant was 
    allowed to operate to potential core power instability, and would not, 
    therefore, have a significant effect ont he margin of safety related to 
    the proposed TS.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: Nicholas S. Reynolds, Esq., Winston & 
    Strawn, 1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: Theodore R. Quay
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: July 29, 1993, with supplemental 
    information provided March 11, 1994 and March 17, 1994
        Description of amendment request: The amendment proposes to modify 
    the Technical Specifications (TS) to reflect a new refueling platform. 
    Specifically, the amendment would add new values for protective 
    features in the TS to reflect the new refueling platform. Values for 
    the old refueling platform are retained in the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The staff's evaluation of the licensee's analysis is 
    presented below:
        1. Does the amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The only accident evaluation affected by the proposed changes are 
    those associated with the Fuel Handling Accident (FHA) analyses 
    presented in WNP-2 Final Safety Analysis Report (FSAR) section 15.7.4. 
    As discussed therein, the fuel handling accident event that produces 
    the largest number of failed spent fuel rods is the drop of a spent 
    fuel bundle into the reactor core when the reactor vessel head is off. 
    The probability of dropping a spent fuel assembly onto other fuel 
    assemblies in the reactor vessel does not increase with the new design. 
    The NF500 mast functions identically to the old mast when grappling, 
    lifting, or moving a fuel assembly. It does not degrade platform design 
    features such as grapple fail-safe on loss of air, dual lifting cables, 
    backup cable reel brake, and the grapple engaged loaded interlock, all 
    of which serve to protect against a fuel drop event. The new mast is 
    more rigid than the previous mast design and, therefore, is less prone 
    to mast bowing. The consequences of dropping a fuel assembly are also 
    unaffected because the weight of the mast is not considered in existing 
    FHA analysis. The number of postulated fuel pins which fail as a result 
    of the FHA is unaffected since the energy imparted by the dropped 
    assembly is independent of the mast design, and mitigating systems will 
    function as previously analyzed. Further, analysis by GE of a 
    postulated accident in which the exposed portion of the NF500 mast is 
    struck by a missile and severed while lifting a fuel bundle with both 
    falling onto the top of the core has been conducted, showing that the 
    consequences of the increased weight of the mast and bundle are bounded 
    by the current WNP-2 FSAR analysis for the fuel bundle only FHA. 
    Retaining the ability to use the old mast does not introduce any 
    changes to the current TS that reflect the analysis of the old mast. 
    The proposed change would not, therefore, significantly increase the 
    probability or consequences of a previously analyzed accident.
        2. Does the amendment create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        No new failure modes are introduced as a result of the proposed 
    changes. The NF500 mast in intended as an exact replacement for the 
    currently installed mast, and is designed to match or exceed the 
    strength and performance of the NF400 mast in all areas. No new fuel 
    handling methods or surveillance procedures will be necessary as a 
    result of installation of the new mast. The proposed change does not 
    affect the manner in which protective interlocks operate. Limits on 
    fuel travel in all directions are unchanged. Retaining the ability to 
    use the NF400 mast presents no new accident possibilities since no 
    changes in fuel mast operation would result from use of the existing 
    mast. The proposed change would not, therefore, create the possibility 
    of a new or different kind of accident from any previously analyzed.
        3. Does the amendment involve a significant reduction in a margin 
    of safety?
        The changed refueling mast cutoff and interlock values account for 
    the increase weight of the mast, or a portion thereof, and do not 
    affect the margins related to the fuel bundle drop analyses. The new 
    mast has the same single failure protection as the old mast. The 
    proposed change would not, therefore, involve a significant reduction 
    in a margin of safety.
        The NRC staff has determined that it appears that the three 
    standards of 50.92(c) are satisfied. Therefore, the NRC staff proposes 
    to determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: Nicholas S. Reynolds, Esq., Winston & 
    Strawn, 1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: Theodore R. Quay
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: December 20, 1993
        Description of amendment request: The amendment proposes to modify 
    the Technical Specifications (TS) to address new containment purge and 
    vent valves to be installed in the 1994 refueling outage. The TS are 
    being modified to remove the requirement to ensure the remaining 
    existing-design valves' position remains at less than or equal to 
    70 deg. because the valves have a permanently installed mechanical stop 
    to limit the open position to ensure adequate closure times. In 
    addition, this modification is being requested because the current TS 
    are too limiting for the new valves, which are designed to close from a 
    90 deg. open position. The TS are also being modified to change the 
    containment leak testing requirements for the new valves from 6 months 
    to 2 years, to reflect the improved seat design of the replacement 
    valves. Additional administrative changes are proposed to delete an 
    out-of-date note, and to relocate an action statement requirement from 
    surveillance section of the TS to the action statements section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
        1. Does the amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Regarding the removal of the requirement to ensure the remaining 
    existing-design valves' position remains at less than or equal to 
    70 deg.: The maximum open position of the containment purge and vent 
    valves is not one of the initiating events for any previously evaluated 
    accident in the WNP-2 FSAR. Thus the proposed change will not affect 
    the probability of an accident previously evaluated. The containment 
    purge and vent valves' position is considered in the accident analyses, 
    and could affect the analyzed consequences of events. The current 
    limiting condition for operation (LCO) and Action Statement requires, 
    and the surveillance verifies, that the permanently installed 70 deg. 
    block is in place and effective. If the existing valves were open 
    further than 70 deg., the valves may not close in time. The valves have 
    a welded mechanical stop installed that limits the position to no more 
    than 70 deg. open, which is a fixed condition that can only be changed 
    by plant modification requiring evaluation against the requirements of 
    10 CFR 50.59. The licensee considers the mechanical stop as sufficient 
    to ensure the existing valves will remain within existing analysis 
    bounds for a design basis loss of coolant accident (LOCA). In addition, 
    the new valves are qualified to close within the 5 seconds assumed in 
    the design basis LOCA. The licensee considers, therefore, that the 
    existing and new valves will operate as required for accident 
    mitigation with the proposed change, and that the proposed change will 
    not affect the consequences of accidents previously evaluated.
        Regarding the modification of the containment leak testing 
    requirements to reflect the new design valves: The containment purge 
    and vent valves are not one of the initiating events for any previously 
    evaluated accident in the WNP-2 FSAR. Thus the proposed change will not 
    affect the probability of an accident previously evaluated. The metal 
    to metal seat valves meet the Appendix J criteria necessary to be 
    tested as type C valves. Type C valves can be tested every 2 years, 
    compared to every 6 months for the current valves. The testing 
    frequency is based on the performance of the valve types to ensure that 
    they are capable of maintaining the necessary leak tightness over the 
    test interval. The new valves' design has been certified to provide the 
    same leak tightness over 2 years that the current valves provide over 6 
    months, thus the consequences of analyzed events remains unaffected by 
    the proposed change.
        Regarding the administrative changes: The proposed change would (1) 
    delete a note that was applicable only through April 10, 1988, and (2) 
    move an action that is currently stated in the SURVEILLANCE 
    REQUIREMENTS section of a TS to the ACTIONS section of the same TS. 
    These changes do not affect the design or operation of the plant or the 
    implementation of the affected TS, and as such would not affect the 
    probability or consequences of previously analyzed events.
        2. Does the amendment create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Regarding the removal of the requirement to ensure the remaining 
    existing-design valves' position remains at less than or equal to 
    70 deg.: No aspect of the design or plant operation is affected by 
    deletion of the surveillance or removal of the reference to the block 
    from the LCO and Action Statement, no new modes of plant operation are 
    introduced, and the proposed change does not require physical 
    modification of the plant. The valves not being replaced will continue 
    to be limited from opening greater than 70 deg. by the welded and non-
    adjustable blocking feature. The capability of these valves to close 
    within 5 seconds to meet the limiting design basis accident (LOCA) will 
    remain unchanged. The replacement valves will be capable of closing 
    within the same 5 seconds from a full-open position of 90 deg.. Since 
    the proposed change does not introduce any new component, system, or 
    plant operating conditions, the change does not create the possibility 
    of a new or different kind of accident from any previously analyzed.
        Regarding the modification of the containment leak testing 
    requirements to reflect the new design valves: The proposed change in 
    surveillance frequency for the replacement valves does not introduce 
    any new mode of plant operation, nor does it involve plant 
    modifications. The new valves operate in the same manner as the old 
    valves, only the seating surfaces are different. This does not affect 
    the way the valves operate to perform their function. The proposed 
    change would not, therefore, involve any new or different kinds of 
    accidents from any previously evaluated.
        Regarding the administrative changes: The proposed changes do not 
    introduce any new modes of plant or equipment operation, nor do they 
    involve physical modification of the plant. The proposed change would 
    not, therefore, create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Does the amendment involve a significant reduction in a margin 
    of safety?
        Regarding the removal of the requirement to ensure the remaining 
    existing-design valves' position remains at less than or equal to 
    70 deg.: The margin of safety of concern with the proposed change is 
    the need for the containment purge and vent valves to close in 5 
    seconds, which will ensure that part 100 limits for design basis events 
    are not exceeded. The proposed change does not affect the maximum open 
    position of the existing valves, thus the valves will still close 
    within 5 seconds. In addition, the new valves, with their maximum full 
    open position of 90 deg., are a new design that will still close within 
    the five seconds from the full open position, thereby preserving the 
    existing margin of safety.
        Regarding the modification of the containment leak testing 
    requirements to reflect the new design valves: The margin of safety 
    involved in the proposed TS change is the amount of leakage that may 
    occur due to plant degradation that may affect the design basis 
    accident assumptions for leakage. The new design valves have been 
    certified to provide the same leak tightness over 2 years that the 
    current valves provide over 6 months, thus the leakage assumptions for 
    design basis events is unaffected. The proposed change would not, 
    therefore, affect the margin of safety provided by the TS.
        Regarding the administrative changes: There are no margins of 
    safety affected by the administrative changes.
        Based on this review, it appears that the three standards of 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: M. H. Philips, Jr., Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: Theodore R. Quay
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: January 6, 1994
        Description of amendment request: The amendment proposes to modify 
    the Technical Specifications (TS) to remove the requirements for the 
    Seismic Monitoring Instrumentation from the TS and relocate them to the 
    FSAR and plant procedures. The requirements described in the 
    specifications will be maintained in the FSAR and plant procedures.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The staff's evaluation of the licensee's analysis is 
    presented below:
        1. Does the amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The seismic monitors only provide monitoring and recording of 
    seismic events that might occur in the vicinity of WNP-2. The 
    instrumentation are not relied upon in current accident analyses for 
    any automatic or manual initiation of safety systems in response to a 
    seismic event. The proposed change would not, therefore, significantly 
    increase the probability or consequences of a previously analyzed 
    accident.
        2. Does the amendment create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not affect the manner in which the plant 
    is operated, maintained, or tested. The proposed change would not, 
    therefore, create the possibility of a new or different kind of 
    accident from any previously analyzed.
        3. Does the amendment involve a significant reduction in a margin 
    of safety?
        The seismic monitors provide monitoring and recording functions 
    only, and are not relied upon in accident analyses for automatic or 
    manual initiation of any safety system. Thus the results of analyzed 
    events, and the associated margins of safety, are unaffected by the 
    administrative removal of the seismic monitors from the TS. The 
    proposed change would not, therefore, involve a significant reduction 
    in a margin of safety.
        The NRC staff has determined that it appears that the three 
    standards of 50.92(c) are satisfied. Therefore, the NRC staff proposes 
    to determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: Nicholas S. Reynolds, Esq., Winston & 
    Strawn, 1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: Theodore R. Quay
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: February 17, 1994
        Description of amendment request: The amendment proposes to modify 
    the Technical Specifications (TS) to support hydrostatic testing of the 
    reactor coolant system. Specifically, the proposed amendment would: (1) 
    add a Special Test Exception that would allow Mode 4 (Cold Shutdown) 
    operation up to 212 deg.F, compared to the current limit of 200 deg.F, 
    without shutdown cooling in operation, to conduct hydrostatic testing, 
    and (2) add a new reactor metal temperature vs reactor vessel pressure 
    (P/T) limit curve that is applicable up to 8 effective full power years 
    (EFPY), for use during hydrostatic testing and non-nuclear plant 
    heatup.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
        1. Does the amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Regarding the proposed Special Test Exception: The proposed change 
    would allow performance of hydrostatic testing in OPERATIONAL CONDITION 
    4 at temperatures greater than 200 deg.F but less than or equal to 
    212 deg.F. Operating in this condition is only allowed if specified 
    OPERATIONAL CONDITION 3 secondary containment requirements are met. The 
    operating condition is not considered as an initiator for any event 
    analyzed in the FSAR, therefore the proposed change would not affect 
    the probability of an accident previously evaluated.
        The specified OPERATIONAL CONDITION 3 requirements compensate for 
    the allowed temperature increase and assure that the consequences of a 
    potential leak will be conservatively bounded by the existing FSAR 
    accident analyses, as discussed below.
        The hydrostatic test is conducted near water solid, all rods in, 
    and temperature less than or equal to 212 deg.F. The stored energy in 
    the core will be very low (approximately 43 days of shutdown conditions 
    and partial core replacement during refueling) and the potential for 
    failed fuel and a subsequent increase in coolant activity above 
    Technical Specification limits is minimal. In addition, secondary 
    containment will be OPERABLE and capable of handling airbone 
    radioactivity from leaks that could occur during the performance of the 
    testing. Maintaining the temperature less than or equal to 212 deg.F 
    will ensure that any leak will not flash to steam, thereby ensuring the 
    potential for airborne activity remains low. Requiring the standby gas 
    treatment system (SGTS) to be OPERABLE will conservatively ensure that 
    any airborne radiation from leaks will be processed by the SGTS thereby 
    limiting releases to the environment. Existing pipe breaks analyzed in 
    Chapter 15 of the FSAR are bounding for the proposed condition. In the 
    event of a large break, the reactor would rapidly depressurize, 
    allowing the low pressure ECCS subsystems to operate. The capability of 
    the subsystems required for OPERATIONAL CONDITION 4 would be adequate 
    to keep the core flooded under this condition. Small system leaks would 
    be detected by leakage inspections before significant inventory loss 
    occurred. Thus the consequences of previously analyzed accidents are 
    not increased by the proposed amendment.
        Regarding the proposed P/T limit curve: The proposed change would 
    modify the P/T limit curves that are based on prevention of brittle 
    fracture of the reactor vessel. The proposed change would result in 
    plant operation closer to the actual brittle fracture condition of the 
    reactor vessel, potentially making a brittle fracture more likely. This 
    condition is offset by the slow heatup conducted using only pump heat, 
    which would result in lower stresses in the reactor vessel than are 
    assumed in the brittle fracture analyses. The resulting P/T limit curve 
    based on 8 EFPY would have sufficient conservatism from the actual 
    vessel brittle fracture condition to make vessel failure as unlikely as 
    the original 32 EFPY curve.
        The potential reactor vessel failure mechanisms are not affected by 
    the proposed change, therefore the consequences of previously analyzed 
    accidents are unaffected by the proposed change.
        2. Does the amendment create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Regarding both the proposed Special Test Exception and the proposed 
    P/T limit curve: The proposed change introduces no new failure modes, 
    involves no physical modification to the plant or change in system 
    configurations, nor does it involve changes in plant, system, or 
    component operation. The proposed change, therefore, does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Does the amendment involve a significant reduction in a margin 
    of safety?
        Regarding the proposed Special Test Exception: The hydrostatic test 
    is conducted with low stored energy in the reactor, which is bounded by 
    the assumed decay heat in current safety analyses. In the unlikely 
    event that a leak from the reactor coolant system were to occur, the 
    RPV would depressurize and the low pressure systems would be available 
    to keep the core flooded. This would ensure that the fuel peak clad 
    temperature would not exceed 2200 deg.F, which is the design basis that 
    provides the margin of safety for the reactor itself. In addition, 
    secondary containment will be maintained during the hydrostatic test, 
    which would ensure that any potential airborne activity that might 
    occur would be filtered through the SGTS. This would ensure that the 
    current margins to the 10 CFR Part 100 limits remain bounded by current 
    analyses. The proposed change would, therefore, not involve a 
    significant reduction in the margins of safety.
        Regarding the proposed P/T limit curve: The proposed new curves 
    would allow plant operation closer to the actual brittle fracture 
    condition of the reactor vessel during hydrostatic test conditions 
    only. This would result in a reduced margin in the protection afforded 
    by the P/T curve. The new curves would, however, allow a lower 
    temperature for conduct of the hydrostatic test, which would increase 
    the heat sink available in the RCS, and increase the margin to decay 
    heat loads assumed in accident analyses. This would result in reduced 
    potential for extensive flow from any break, reduce the time for 
    initiation of low pressure ECCS systems, and reduce the available 
    radioactive decay products that are available for release during any 
    postulated accident condition. The overall impact of the conditions 
    increases the margin to 10 CFR Part 100 limits that are the design 
    margin of safety for postulated loss of coolant accidents. The overall 
    effect of the proposed change would not involve a significant reduction 
    in the overall margins of safety.
        Based on this review, it appears that the three standards of 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: M. H. Philips, Jr., Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: Theodore R. Quay
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: February 23, 1994
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    6.8.c by removing the requirement to conduct a biennial review of plant 
    procedures in accordance with American National Standards Institute 
    (ANSI) N18.7-1976. The licensee proposes using alternate programs, that 
    are already in place, to ensure that procedures are periodically 
    reviewed and maintained current. A biennial review of the Integrated 
    Plant Emergency Operating Procedures (IPEOPs), however, would continue. 
    The requirements for these alternate programs and for the IPEOP review 
    would be added to the Operational Quality Assurance Program Description 
    (OQAPD).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The likelihood that an accident will occur is neither increased 
    or decreased by eliminating the periodic reviews of routine 
    administrative and technical procedures. Sufficient controls are 
    established to ensure that procedures impacting safety-related 
    structures, systems, and components are maintained current, 
    accurate, and usable. This TS change will therefore not impact the 
    function or method of operation of plant equipment. Thus, a 
    significant increase in the probability of a previously analyzed 
    accident does not result due to this change. No systems, equipment, 
    or components are affected by the proposed changes. Thus, the 
    consequences of a malfunction of equipment important to safety 
    previously evaluated in the Updated Safety Analysis Report (USAR) 
    are not increased by this change. The proposed changes do not affect 
    equipment or its operation, and, thus, do not affect the 
    probabilities or consequences of an accident. Therefore, WPSC 
    concludes that this change does not significantly increase the 
    probability or consequences of an accident.
        2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes do not involve changes to the physical 
    plant or operations. Since periodic procedure reviews do not 
    contribute to accident initiation, a change related to such an 
    activity does not produce a new accident scenario or produce a new 
    type of equipment malfunction. Also, this change does not alter any 
    existing accident scenarios. The proposed changes do not affect 
    equipment or its operation, and thus, do not increase the 
    possibility of a new or different kind of accident.
        3) involve a significant reduction in the margin of safety.
        The proposed changes do not affect equipment or its operation, 
    and thus, do not involve any reduction in the margin of safety. 
    Therefore, use of the proposed Technical Specification would not 
    involve any reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: John N. Hannon
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendment: February 17, 1994
        Brief description of amendment request: The proposed amendments 
    would revise the combined Technical Specifications (TS) for the Diablo 
    Canyon Power Plant Unit Nos. 1 and 2 to revise TS 3/4.3.2, ``Engineered 
    Safety Feature Actuation System Instrumentation,'' as follows: (1) 
    Table 3.3-3, functional unit 6.c.2), channels to trip, would be changed 
    from 2/steam generator in one steam generator to 2/steam generator in 
    any 2 steam generators to correct an administrative error. (2) Table 
    3.3-4 would be changed as follows: a. functional unit 4.6., Negative 
    Steam Pressure Rate - High, trip setpoint and allowable value, would be 
    changed from -100 psi/sec and -105.4 psi/sec to 100 psi and 105.4 psi, 
    respectively; b. a note would be added stating that the time constants 
    utilized in the rate-lag controller for Negative Steam Pressure Rate - 
    High, are equal to 50 seconds.
        Date of individual notice in Federal Register: March 1, 1994 (59 FR 
    9789)
        Expiration date of individual notice: March 31, 1994
        Local Public Document Room location: California Polytechnical State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: March 4, 1994
        Brief description of amendment request: The proposed amendment 
    would add a new Section 3/4.10.8, ``Inservice Leak and Hydrostatic 
    Testing,'' and the Bases. The new section would allow Hope Creek to 
    remain in OPERATIONAL CONDITION 4 with reactor coolant temperatures up 
    to 212 *F to facilitate inservice leak and hydrostatic testing.
        Date of publication of individual notice in Federal Register: March 
    16, 1994 (59 FR 12384)
        Expiration date of individual notice: April 15, 1994
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: April 28, August 12, and November 17, 
    1993, and February 2, 1994
        Brief description of amendment request: The proposed changes 
    increase the spent fuel pool capacities for Salem 1 and 2 from the 
    current 1170 fuel assemblies to 1632 fuel assemblies. Also, the decay 
    time for refueling operations is being extended from 100 hours to 168 
    hours.
        Date of publication of individual notice in Federal Register: March 
    4, 1994 (59 FR 10440)
        Expiration date of individual notice: April 4, 1994
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket No. 50-317, Calvert 
    Cliffs Nuclear Power Plant, Unit No. 1, Calvert County, Maryland
    
        Date of application for amendment: September 3, 1993, as 
    supplemented February 1, 1994
        Brief description of amendment: The amendment revises the heatup 
    and cooldown curves and the low-temperature overpressure protection 
    (LTOP) controls. The changes to the LTOP controls support proposed 
    modifications to allow a variable-setpoint (VLTOP) protection system. 
    The VLTOP system will increase the allowable operating pressure band in 
    the LTOP region and increase the flexibility in the use of the reactor 
    coolant pumps.
        Date of issuance: March 15, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 185
        Facility Operating License No. DPR-53: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 29, 1993 (58 
    FR 50963) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 15, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: September 17, 1993, as 
    supplemented on January 4, 1994
        Brief description of amendments: The amendments implement the 
    recommendations provided in Generic Letter 88-16, ``Removal of Cycle-
    Specific Parameter Limits From Technical Specifications,'' by removing 
    cycle specific values from the Technical Specifications (TSs) and 
    incorporating them in a separate document. The amendments also include 
    two other changes. One is the removal of outdated references to power 
    operation with less than four reactor coolant pumps in operation and 
    the other includes administrative changes to clarify the existing TSs, 
    but do not alter the existing requirements.
        Date of issuance: March 17, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 186 and 163
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 27, 1993 (58 FR 
    57844) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated March 17, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: August 27, 1993, as 
    supplemented February 21, 1994
        Brief description of amendments: The amendments revise the 
    requirements for snubber visual inspection intervals and corrective 
    actions in accordance with Generic Letter 90-09. The amendments also 
    remove two of the options for determining the sample size to be used 
    for snubber functional testing.
        Date of issuance: March 11, 1994
        Effective date: March 11, 1994
        Amendment Nos.: 60, 60, 48, and 48
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4935) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 11, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: June 1, 1992
        Brief description of amendments: The amendments update the leakage 
    test requirements of the drywell airlock to the standards of 10 CFR 
    Part 50, Appendix J, Section III.D.2.
        Date of issuance: March 11, 1994
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 125, 119, 145, and 141
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29, and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: October 28, 1992 (57 FR 
    48818) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 11, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Dresden, The Morris Public 
    Library, 604 Liberty Street, Morris, Illinois 60450; for Quad Cities, 
    The Dixon Public Library, 221 Hennepin Avenue, Dixon, Illinois 61021.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: February 25, 1993
        Brief description of amendments: The amendments change Technical 
    Specification 4.8.1.1.2.c to update the diesel fuel oil testing 
    requirements to the standards of ASTM D4057-88 (new fuel oil test); 
    ASTM D975-88 (water and sediment content testing); and ASTM D2276-89 
    (impurity levels). The updated standards will be referenced in the 
    Technical Specification Bases.
        Date of issuance: March 10, 1994
        Effective date: March 10, 1994
        Amendment Nos.: 97 and 81
        Facility Operating License Nos. NPF-11 and NPF-18. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36431) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 10, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: October 28, 1993, supplemented 
    by letter dated January 21, 1994.
        Brief description of amendments: The amendments revise the ECCS 
    injection valve stroke times and ECCS response times to allow the 
    licensee to perform Motor Operated Valve modifications that slow down 
    injection valve stroke times. As part of this change, a limited break 
    spectrum Loss-Of-Coolant Accident analysis was performed to evaluate 
    the impact of the slower response on the Peak Cladding Temperatures and 
    to update the plants licensing bases.
        Date of issuance: March 9, 1994
        Effective date: March 9, 1994
        Amendment Nos.: 96 and 80
        Facility Operating License Nos. NPF-11 and NPF-18. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4937) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 9, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad 
    Cities Nuclear Power Station, Units 1 and 2, Rock Island County, 
    Illinois
    
        Date of application for amendments: October 21, 1993
        Brief description of amendments: The amendments delete the 
    requirements for demonstrating the operability of redundant equipment 
    when emergency core cooling system equipment is found to be inoperable, 
    or made inoperable for maintenance. The changes are consistent with the 
    guidance provided by the NRC staff in Generic Letter 93-05, dated 
    September 27, 1993.
        Date of issuance: March 8, 1994
        Effective date: March 8, 1994
        Amendment Nos.: 144 and 140
        Facility Operating License Nos. DPR-29 and DPR-30. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59747) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 8, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Mississippi Power & 
    Light Company, Docket No. 50-416, Grand Gulf Nuclear Station, Unit 
    1, Claiborne County, Mississippi
    
        Date of application for amendment: April 21, 1993
        Brief description of amendment: This amendment deleted License 
    Condition 2.C(36), Attachment 1, Item (c)(4) which implemented the 
    requirements of Regulatory Guide 1.97, ``Instrumentation For Light-
    Water-Cooled Nuclear Power Plants to Assess Plant and Environs 
    Conditions During and Following an Accident,'' for the Grand Gulf 
    Nuclear Station because analysis shows that these requirements are 
    being met by alternative methods.
        Date of issuance: March 7, 1994
        Effective date: March 7, 1994
        Amendment No: 112
        Facility Operating License No. NPF-29. Amendment revises the 
    license.
        Date of initial notice in Federal Register: May 12, 1993 (58 FR 
    28056) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 7, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Judge George W. Armstrong 
    Library, Post Office Box 1406, S. Commerce at Washington, Natchez, 
    Mississippi 39120.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: May 8, 1991, as supplemented by letters 
    dated March 6, 1992, and January 28, 1993
        Brief description of amendment: The amendment revised the Technical 
    Specifications by revising the fuel oil amounts in the feed and storage 
    tanks for the emergency diesel generators, clarifying the testing for 
    the interconnecting piping, and revising the specific gravity of the 
    fuel oil.
        Date of issuance: March 16, 1994
        Effective date: March 16, 1994
        Amendment No.: 92
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 26, 1991 (56 FR 
    29274), as revised April 14, 1993 (58 FR 19478) The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated March 16, 1994. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: June 21, 1993
        Brief description of amendments: These amendments will change 
    Technical Specifications Section 6.0, ``Administrative Controls,'' by 
    (a) revising unit staff titles to those of the current FPL Nuclear 
    Division organization, (b) revising the composition of the Facility 
    Review Group (FRG) to broaden the scope of available expertise, and (c) 
    making minor editorial corrections.
        Date of issuance: March 2, 1994
        Effective date: March 2, 1994
        Amendment Nos.: 126, 65
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 21, 1993 (58 FR 
    39050) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 2, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: August 17, 1993, as 
    supplemented January 14, 1994.
        Brief description of amendments: These amendments relocate fire 
    protection requirements from the Technical Specifications to the Final 
    Safety Analysis Report in accordance with Generic Letter 86-10, 
    ``Implementation of Fire Protection Requirements,'' and amend the 
    license conditions accordingly.
        Date of issuance: February 25, 1994
        Effective date: February 25, 1994
        Amendment Nos. 159 and 153
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Licenses and Technical Specifications.
        Date of initial notice in Federal Register: September 29, 1993 (58 
    FR 50967) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated February 25, 1994. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: December 16, 1993
        Brief description of amendment: The amendment revises the Technical 
    Specifications to clarify the requirements for maintaining secondary 
    containment integrity when one or more Reactor Building Ventilation 
    supply and exhaust valves are declared inoperable. The Technical 
    Specifications add a new Limiting Condition for Operation, Basis 
    Statement and Surveillance Requirements for these isolation valves.
        Date of issuance: March 7, 1994
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 168
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4938) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated March 7, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, New Jersey 
    08753.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: August 26, 1993
        Brief description of amendment: The amendment revises the plant 
    Technical Specifications (TSs) to accommodate limited fuel 
    reconstitution based on NRC Generic Letter (GL) 90-02, Supplement 1. 
    Such reconstitution may be appropriate in the event of a leaking fuel 
    rod, in which case the fuel rod would be replaced with a stainless 
    steel or zirconium alloy filler rod.
        Date of issuance: March 15, 1994
        Effective date: As of its date of issuance, to be implemented 
    within 30 days of issuance.
        Amendment No.: 183
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59751). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 15, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: April 16, 1991, as supplemented 
    January 6, 1993.
        Brief description of amendments: The amendments revise the 
    technical specifications to incorporate recommendations from NRC 
    Generic Letter 90-06 for power-operated relief valve and block valve 
    reliability and low-temperature overpressure protection.
        Date of issuance: March 9, 1994
        Effective date: March 9, 1994
        Amendment Nos.: 176 & 161
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 3, 1993 (58 FR 
    12261) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 9, 1994
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: January 25, 1993, as 
    supplemented by letters dated November 3 and 23, and December 9, 1993, 
    and January 5 and 24, 1994.
        Brief description of amendment: This amendment increases the 
    maximum number of spent fuel assemblies that can be stored in the Maine 
    Yankee fuel pool to 2019 from 1476. The increase in fuel storage 
    capacity is required so that storage space is available for spent fuel 
    through the duration of the current operating license, including the 
    final full core offload.
        Date of issuance: March 15, 1994
        Effective date: March 15, 1994
        Amendment No.: 144
        Facility Operating License No. DPR-36: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1993 (58 FR 
    16423) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 15, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, Maine 04578.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of application for amendment: December 22, 1993
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.4.4.e (Emergency Ventilation System) to permit 
    fuel handling operations to continue during refueling beyond 7 days 
    with one circuit of the emergency ventilation system inoperable, 
    provided the remaining emergency ventilation system circuit is operable 
    and in operation. The change to TS 3.4.4.e is consistent with the NRC's 
    Improved Standard Technical Specifications, NUREG-1433.
        Date of issuance: March 8, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 146
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4940) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 8, 1994. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of application for amendment: December 27, 1993
        Brief description of amendment: The amendment relocates TS Tables 
    3.2.7, ``Reactor Coolant Isolation Valves,'' and 3.3.4, ``Primary 
    Containment Isolation Valves,'' from TSs 3.2.7/4.2.7 and 3.3.4/4.3.4, 
    respectively, to a plant procedure which governs lists removed from TSs 
    per Generic Letter (GL) 91-08, ``Removal of Component Lists from 
    Technical Specifications.'' The plant procedure would be subject to the 
    requirements specified in the Administrative Controls section of the 
    NMP-1 TSs. The proposed amendment would also make conforming changes to 
    the TS Bases. These lists of valves will continue to be included in the 
    NMP-1 Updated Final Safety Analysis Report. Relocation of these valve 
    lists from the NMP-1 TSs to the plant procedure is consistent with NRC 
    staff guidance issued in GL 91-08.
        Date of issuance: March 7, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 145
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4941) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 7, 1994. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: June 11, 1993, supplemented by 
    letter dated November 15, 1993.
        Brief description of amendment: The amendment revises the pressure/ 
    temperature (P/T) limits for the reactor vessel. Specifically, Figure 
    3.4-2, ``Millstone Unit 2 Reactor Coolant System Pressure-Temperature 
    Limitations for 12 Full Power Years,'' on page 3/4 4-19, is revised to 
    reflect the change in the curves and the title change to ``Millstone 
    Unit 2 Reactor Coolant System Pressure-Temperature Limitations for 20 
    EFPY.''
        Date of issuance: January 27, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 170
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 21, 1993 (58 FR 
    39054) The November 15, 1993, submittal provided information that did 
    not change the initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated January 27, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: May 7, 1993
        Description of amendment request: The amendment changes Technical 
    Specification (TS) 3/4 6.1 relating to primary containment integrity. 
    Limiting Condition for Operation (LCO) 3.6.1.7 is changed to delete the 
    requirements applicable to the 36-inch containment shutdown purge 
    supply and exhaust isolation valves in the containment air purge (CAP) 
    system. Surveillance Requirement (SR) 4.6.1.7.1 and associated footnote 
    and SR 4.6.1.7.2 are deleted also. To maintain document consistency, 
    certain other editorial changes were made.
        Date of issuance: March 7, 1994
        Effective date: Not effective until operational MODE 5 is entered 
    when commencing the third refueling outage, and is to be implemented 
    prior to reentering operational MODE 4.
        Amendment No.: 29
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34083). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 7, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 47 
    Front Street, Exeter, New Hampshire 03833.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: July 7, 1993
        Brief description of amendments: The amendments revise the combined 
    Technical Specifications (TS) for the Diablo Canyon Power Plant Unit 
    Nos. 1 and 2 to change TS 5.1.3, ``Map Defining Unrestricted Areas and 
    Site Boundary for Radioactive Gaseous and Liquid Effluents,'' to be 
    consistent with a recent interpretation of the restricted area 
    definition in 10 CFR 20.
        Date of issuance: March 3, 1994
        Effective date: March 3, 1994
        Amendment Nos.: 90 & 89
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 18, 1993 (58 FR 
    43930) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 3, 1994, and an 
    environmental assessment was published in the Federal Register on 
    February 25, 1994, (59 FR 9252). No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: September 8, 1993 (Reference 
    LAR 93-06)
        Brief description of amendments: The amendments revise the combined 
    Technical Specifications (TS) for the Diablo Canyon Power Plant Unit 
    Nos. 1 and 2. Specifically, TS 1.44, ``Radiological Monitoring and 
    Controls Program,'' 3/4.11, ``Radioactive Effluents,'' and 6.14, 
    ``Radiological Monitoring and Controls Program (RMCP), Offsite Dose 
    Calculation Procedure (ODCP) and Environmental Radiological Monitoring 
    Procedure (ERMP),'' are revised to change the Semiannual Radioactive 
    Effluent Release Report to Annual Radioactive Effluent Release Report. 
    The amendment also revises TS 6.2.3, ``Onsite Safety Review Group 
    (OSRG),'' 6.5.2, ``Plant Staff Review Committee,'' and 6.5.3.7, 
    ``Nuclear Safety Oversight Committee Review,'' to implement 
    organizational changes.
        Date of issuance: March 7, 1994
        Effective date: March 7, 1994
        Amendment Nos.: 91 and 90
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 27, 1993 (58 FR 
    57855) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 7, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: October 8, 1993
        Brief description of amendments: The amendments revised the 
    existing definition of CHANNEL CALIBRATION in Technical Specification 
    1.4 to allow in-place qualitative methods to be used to verify 
    resistance temperature detector or thermocouple sensor behavior.
        Date of issuance: March 8, 1994
        Effective date: March 8, 1994
        Amendment Nos.: 133 and 102
        Facility Operating License Nos. NPF-14 and NPF-22. These amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59754) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 8, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company Delmarva Power and Light Company, and Atlantic City 
    Electric Company, Docket Nos. 50-277 and 50-278, Peach Bottom 
    Atomic Power Station, Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 1, 1993 as 
    supplemented January 26, 1994 and February 18, 1994.
        Brief description of amendments: These amendments concern the 
    Radiation Monitoring Systems - Isolation and Initiation Functions of 
    the Technical Specifications and are necessary to support modification 
    5281. This modification replaces the obsolete control room ventilation 
    radiation monitoring equipment.
        Date of issuance: March 15, 1994
        Effective date: March 15, 1994
        Amendments Nos.: 184 and 189
        Facility Operating License Nos. DPR-44 and DPR-56: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64614) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 15, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: July 15, 1993
        Brief description of amendment: The amendment revises the Technical 
    Specifications to eliminate the reactor scram and Main Steam Line 
    Isolation Valve closure requirements associated with the Main Steam 
    Line Radiation Monitors. The changes are consistent with Licensing 
    Topical Report NEDO-31400, ``Safety Evaluation for Eliminating the 
    Boiling Water Reactor Main Steam Isolation Valve Closure Function and 
    Scram Function of the Main Steam Line Radiation Monitor,'' dated May 
    1987.
        Date of issuance: March 9, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 207
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41513) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 9, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: October 16, 1992
        Brief description of amendments: These amendments revise TS 3/
    4.3.4, ``Turbine Overspeed Protection,'' to allow one surveillance 
    every 31 days for verification of turbine overspeed protection system 
    operability. Currently, the surveillance tests are performed at power 
    every 7 days and again every 31 days. The 31-day test is performed by 
    an operator with an observer at the valve.
        Date of issuance: March 9, 1994
        Effective date: March 9, 1994
        Amendment Nos.: 111 and 100
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 17, 1993 (58 
    FR 8783) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 9, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: January 10, 1992 (TS304)
        Brief description of amendments: The amendments address emergency 
    diesel generator availability for the plant shared systems of Standby 
    Gas Treatment and Control Room Emergency Ventilation.
        Date of issuance: March 9, 1994
        Effective date: March 9, 1994
        Amendment Nos.: 203, 222 and 176
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 15, 1992
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 9, 1994. No significant hazards 
    consideration comments received: None
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: January 8, 1993; which was 
    supplemented by submittals dated April 1, May 3, and August 18, 1993; 
    and February 22, 1994.
        Brief description of amendments: The amendments remove the 
    surveillance requirement to perform reactor vessel nozzle inspections 
    at the end of each 10-year inspection interval.
        Date of issuance: March 15, 1994
        Effective date: March 15, 1994
        Amendment Nos.: 177 and 168
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: February 3, 1993 (58 FR 
    7007) The Commission's related evaluation of the amendments are 
    contained in a Safety Evaluation dated March 15, 1994. No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
    
        Date of application for amendments: July 2, 1993, as supplemented 
    December 10, 1993
        Brief description of amendments: These amendments modify the 
    Technical Specifications having cycle-specific parameters limits by 
    replacing the values of those limits with a reference to a Core 
    Operating Limits Report for the values of those limits.
        Date of issuance: March 2, 1994
        Effective date: March 2, 1994
        Amendment Nos. 189 and 189
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41519) The December 10, 1993, submittal did not expand the scope of the 
    original application and did not change the proposed no significant 
    hazards determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated March 2, 1994. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185
    
    Virginia Electric and Power Company, Docket Nos. 50-280, 50-281, 
    50-338, and 50-339, Surry Power Station, Unit Nos. 1 and 2, Surry 
    County, Virginia, and North Anna Power Station, Unit Nos. 1 and 2, 
    Louisa County, Virginia.
    
        Date of application for amendments: July 20, 1993
        Brief description of amendments: These amendments delete the 
    Technical Specifications requirement for Station Nuclear Safety and 
    Operating Committee review of the Emergency and Security Plans. This 
    requirement remains in the respective plans. The audit frequencies are 
    also being deleted from the TS.
        Date of issuance: March 1, 1994
        Effective date: March 1, 1994
        Amendment Nos. 188, 188, (Surry 1&2) 180, 161 (North Anna 1&2)
        Facility Operating License Nos. DPR-32, DPR-37, NPF-4 and NPF-7: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46242) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 1, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room locations: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185, and The Alderman 
    Library, Special Collections Department, University of Virginia, 
    Charlottesville, Virginia 22903-2498.
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
    
        Date of application for amendments: December 10, 1993
        Brief description of amendments: These amendments modify the 
    surveillance requirements for the Auxiliary Feedwater System pumps and 
    valves, define ``staggered test basis,'' and make administrative 
    changes to the Technical Specifications.
        Date of issuance: March 7, 1994
        Effective date: March 7, 1994
        Amendment Nos. 190 and 190
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 19, 1994 (59 FR 
    2873) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 7, 1994. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By April 29, 1994, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: February 25, 1994 as 
    supplemented on March 11, 1994
        Brief description of amendment: The amendment revised the Technical 
    Specifications by adding a footnote to Specification 3/4.4.3.1, 
    ``Reactor Coolant System Leakage - Leakage Detection Systems,'' to 
    permit continued plant operations with inoperable drywell floor drain 
    sump flow monitoring instrumentation until the first time the plant is 
    required to be brought to COLD SHUTDOWN after March 15, 1994.
        Date of issuance: March 14, 1994
        Effective date: March 14, 1994
        Amendment No.: 89
        Facility Operating License No. NPF-62. The amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazardsconsideration: No.
        The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated March 
    14, 1994.
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Indiana Michigan Power Company, Docket No. 50-315, Donald C. Cook, 
    Nuclear Plant, Unit No. 1, Berrien County, Michigan
    
        Date of application for amendment: December 15, 1993, as 
    supplemented February 15 and 24, 1994 (December 15, 1993, application 
    supersedes the licensee's March 10, 1993 application.)
        Brief description of amendment: The amendment revises the Technical 
    Specifications to allow the continuance of voltage-based steam 
    generator tube plugging criteria for outside-diameter stress corrosion 
    cracking at tube support plate elevations. The amendment allows the use 
    of a 2.0 volt interim repair criterion for Cycle 14 operation.
        Date of issuance: March 15, 1994
        Effective date: March 15, 1994
        Amendment No.: 178
        Facility Operating License No. DPR-58. Amendment revises the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration. Yes. The December 15, 1993, 
    application was noticed in the Federal Register on January 5, 1994 (59 
    FR 621). The NRC also published a public notice of the proposed 
    amendment, issued a proposed finding of no significant hazards 
    consideration, and requested that any comments on the proposed finding 
    be provided to the staff by the close of business on March 7, 1994. The 
    notice was published in the South Haven Tribune on March 1, 1994, and 
    in the Herald-Palladium on March 2, 1994. No comments have been 
    received.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultation with the State of Michigan, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 15, 1994.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        NRC Project Director: Ledyard B. Marsh
    
    Indiana Michigan Power Company, Docket No. 50-315, Donald C. Cook, 
    Nuclear Plant, Unit No. 1, Berrien County, Michigan
    
        Date of application for amendment: February 15, 1994
        Brief description of amendment: The amendment revises the Technical 
    Specifications
        Date of issuance: March 14, 1994
        Effective date: March 14, 1994
        Amendment No.: 177
        Facility Operating License No. DPR-58. Amendment revises the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration. Yes. The NRC published a public 
    notice of the proposed amendment, issued a proposed finding of no 
    significant hazards consideration, and requested that any comments on 
    the proposed finding be provided to the staff by the close of business 
    on March 7, 1994. The notice was published in the South Haven Tribune 
    on March 1, 1994, and in the Herald-Palladium on March 2, 1994. No 
    comments have been received.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultantion with the State of Michigan, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 14, 1994
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        NRC Project Director: Ledyard B. Marsh
        Dated at Rockville, Maryland, this 23rd day March 1994.
        For the Nuclear Regulatory Commission.
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation
    [Doc. 94-7331 Filed 3-29-94; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
03/30/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
X94-20330
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: March 30, 1994