96-8786. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 70 (Wednesday, April 10, 1996)]
    [Notices]
    [Pages 15985-16005]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-8786]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 16, 1996, through March 29, 1996. The 
    last biweekly notice was published on March 27, 1996 (61 FR 13521).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S.
    
    [[Page 15986]]
    
    Nuclear Regulatory Commission, Washington, DC 20555, and should cite 
    the publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By May 10, 1996, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: September 30, 1994, as supplemented 
    September 18, 1995, January 19 and March 15, 1996
        Description of amendment request: Currently, the steam generators 
    (SGs) in place in the Catawba units are Westinghouse Model ``D'' type 
    preheat SGs. The tube degradation levels in the SGs at Catawba Unit 1 
    have affected the reliability of the unit. Therefore, these generators 
    are scheduled to be replaced with feedring SGs designed by Babcock
    
    [[Page 15987]]
    & Wilcox International. The design differences and analysis changes to 
    support the feedring SGs result in the need to change the Technical 
    Specifications (TS) in the following areas: (a) revise low-low SG water 
    level for the reactor trip setpoint in TS Table 2.2-1 and for auxiliary 
    feedwater actuation in TS Table 3.3-4, (b) revise high-high SG water 
    level setpoint for turbine trip and feedwater isolation in TS Table 
    3.3-4, (c) delete reference to SG tube repair methods which will no 
    longer be applicable after the replacement of the SGs and clarify 
    initial surveillances, (d) revise reactor coolant system volume, (e) 
    update Topical Report revision numbers in the Administrative Controls 
    Section 6.9 of the TS, and (f) change the nominal average temperature 
    in TS Table 2.2-1 for the reactor trip system setpoints to reflect the 
    value incorporated into the safety analyses for the replacement SGs. 
    The change made in the September 30, 1994, submittal, to reduce the 
    steam line safety valve lift settings in TS Table 3.7-2, was withdrawn 
    in the September 18, 1995, submittal. The January 19, 1996, submittal 
    proposed changes to reflect the NRC's approved revisions to Topical 
    Reports DPC-NE-3000 and DPC-NE-3002. The March 15, 1996, submittal 
    provided additional information in response to NRC staff requests and 
    also updated and clarified the involved TS pages including changes made 
    to these TS pages by license amendments issued on other topics since 
    the original application dated September 30, 1994.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Operation of Catawba Unit 1 in accordance with the proposed 
    changes to the Technical Specifications will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated. The low-low steam generator water 
    level reactor trip setpoint, the high-high steam generator water 
    level setpoint for turbine trip and feedwater isolation, and the 
    low-low steam generator water level setpoint for auxiliary feedwater 
    initiation are changing to support operation with the replacement 
    steam generators. These setpoints were chosen both to optimize plant 
    operation, and ensure that all applicable acceptance criteria are 
    met for licensing basis safety analysis. These setpoints do not 
    contribute to the initiation of any accident evaluated in the 
    Catawba FSAR [Final Safety Analysis Report] and have no adverse 
    impact on system operation, therefore it can be concluded that these 
    changes will not significantly increase the probability or 
    consequences of an accident evaluated in the FSAR.
        The increase in Reactor Coolant System volume due to the 
    replacement steam generators will not increase the probability or 
    consequences of an accident previously evaluated. The increase in 
    volume has no effect on the probability of occurrence of any 
    accident evaluated in the FSAR. The mass and energy release inside 
    containment due to postulated loss of coolant accidents inside 
    containment has been analyzed to ensure that the peak containment 
    pressure limit is not exceeded. All Chapter 15 reanalysis which was 
    required due to the replacement steam generators assumed the new 
    Reactor Coolant System volume. Since the results of these analyses 
    show the applicable acceptance criteria continue to be met, it can 
    be concluded that the consequences of an accident previously 
    evaluated are not significantly increased due to this change.
        Operation of Catawba Unit 1 in accordance with the proposed 
    changes to the Technical Specification will not create the 
    possibility of a new or different accident from any accident 
    previously evaluated. The proposed changes to revise the low-low 
    steam generator water level reactor trip setpoint, high-high steam 
    generator water level setpoint for turbine trip and feedwater 
    isolation, and low-low steam generator water level setpoint for 
    auxiliary feedwater initiation ensure that the appropriate 
    acceptance criteria for FSAR Chapter 15 transients which rely on 
    these functions are met for operation with the replacement steam 
    generators. ... The increase in Reactor Coolant System volume is 
    taken into account in the analysis of the mass and energy release 
    due to a postulated loss of coolant inside containment, and Chapter 
    15 events which have been reanalyzed due to replacement of the steam 
    generators. As discussed above, the proposed changes will not 
    introduce the possibility of a new or different accident from any 
    previously evaluated, they will ensure that transients that take 
    credit for these functions and dose analyses meet applicable 
    acceptance criteria for operation with the replacement steam 
    generators.
        Operation of Catawba Unit 1 in accordance with the proposed 
    changes to the Technical Specifications will not involve a 
    significant reduction in a margin of safety. The proposed changes 
    were made to ensure that transients that rely on low-low steam 
    generator water level reactor trip setpoint, high-high steam 
    generator water level setpoint for turbine trip and feedwater 
    isolation, and low-low steam generator water level setpoint for 
    auxiliary feedwater actuation meet applicable acceptance criteria. 
    ... The proposed change in the Reactor Coolant System volume will 
    not involve a significant reduction in a margin of safety. The 
    increased volume affects the mass and energy release due to a 
    postulated loss of coolant accident inside containment and the other 
    Chapter 15 events which were reanalyzed due to replacement of the 
    steam generators. This event has been analyzed and the results are 
    within current acceptable limits. As discussed above, the acceptance 
    criteria for FSAR transients which are affected by these proposed 
    changes continue to be met, therefore there is no significant 
    reduction in the margin of safety.
        Changes to the steam generator surveillance requirements will 
    simply delete inspection requirements which are no longer applicable 
    after installation of the replacement steam generators. References 
    to F* criteria, interim plugging criteria, and sleeving are deleted 
    since these repair criteria were approved for use on the current 
    steam generators. Since these changes only delete criteria which 
    will no longer be applicable and cannot be used, no significant 
    hazards considerations are involved.
        The changes to Technical Specification 6.9.1.9 are 
    administrative in nature. These changes are being made to reflect 
    the most recent revisions of DPC-NE-3002 and DPC-NE-3000, which 
    includes changes associated with the replacement steam generators. 
    These topical report revisions [have been] reviewed and approved for 
    use regarding McGuire and Catawba Nuclear Stations. Since these 
    changes are administrative in nature, no significant hazards 
    considerations are involved.
        The proposed change to Technical Specifications [average coolant 
    temperature in Table 2.2-1] does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Changing the value for [the average coolant temperature] 
    in Notes 1 and 3 of Table 2.2-1 will update the value to agree with 
    [the average coolant temperature] assumed in the applicable safety 
    analyses for replacement of the steam generators. Acceptable results 
    were obtained for all required reanalyses. The probability of an 
    accident will not be significantly affected by operation with the 
    new [average coolant temperature] value, because all equipment will 
    be operated within acceptable design limits. The consequences of 
    previously evaluated accidents which are affected by this change 
    have been evaluated, and have been determined to be within 
    acceptable limits.
        This proposed change [to TS Table 2.2-1] will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated. This change does not change the physical 
    configuration of the plant, and all analyses which are affected by 
    replacement of the steam generators have been determined to have 
    acceptable results assuming this value for [average coolant 
    temperature].
        This proposed change to the Technical Specifications [Table 2.2-
    1] will not involve a significant reduction in the margin of safety. 
    All safety analyses which were affected by replacement of the steam 
    generators assumed this value for [average coolant temperature] and 
    the results were determined to be within previously acceptable 
    limits.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    [[Page 15988]]
    
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: January 12, 1996, as supplemented March 
    4, 1996
        Description of amendment request: This request was previously 
    published in the Federal Register on January 31, 1996 (61 FR 3498). It 
    is being renoticed to provide clarification to the scope of the 
    original request. Compliance with 10 CFR Part 50, Appendix J, provides 
    assurance that the primary containment, including those systems and 
    components that penetrate the primary containment, do not exceed the 
    allowable leakage rate values specified in the Technical Specifications 
    (TS) and Bases. The allowable leakage rate is determined so that the 
    leakage assumed in the safety analyses is not exceeded.
        On September 12, 1995, the NRC approved issuance of a revision to 
    10 CFR Part 50, Appendix J, which was subsequently published in the 
    Federal Register on September 26, 1995, and became effective on October 
    26, 1995. The revision added Option B ``Performance-Based 
    Requirements'' to Appendix J to allow licensees to voluntarily replace 
    the prescriptive testing requirements of Appendix J with testing 
    requirements based on both overall and individual component leakage 
    rate performance.
        Regulatory Guide 1.163, ``Performance-Based Containment Leak Test 
    Program,'' was developed as a method acceptable to the staff for 
    implementing Option B. Accordingly, the licensee has submitted, in its 
    application dated January 12, 1996, proposed changes to the TS to 
    implement 10 CFR Part 50, Appendix J, Option B, by referring to 
    Regulatory Guide (RG) 1.163, ``Performance-Based Containment Leakage-
    Test Program.'' Although the licensee's proposal indicated that it was 
    consistent with RG 1.163, it did not include the clarifying changes to 
    the TS that would require the visual examination of containment systems 
    to be consistent with the guidance of RG 1.163. The licensee submitted 
    a supplement, dated March 4, 1996, to its January 12, 1996 proposal, 
    which proposes such changes to TS Surveillance Requirements 4.6.1.6 and 
    4.6.1.7 and associated Bases.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Containment leak rate testing is not an initiator of any 
    accident; the proposed change does not affect reactor operations or 
    accident analysis, and has no significant radiological consequences. 
    Therefore, this proposed change will not involve an increase in the 
    probability or consequences of any previously-evaluated accident.
        2. The proposed change will not create the possibility of any 
    new not previously evaluated.
        The proposed change does not affect normal plant operations or 
    configuration, nor does it affect leak rate test methods. The test 
    history at Catawba (no ILRT [integral leak rate test] failures) 
    provides continued assurance of the leak tightness of the 
    containment structure.
        3. There is no significant reduction in a margin of safety.
        The proposed changes are based on NRC-accepted provisions, and 
    maintain necessary levels of reliability of containment integrity. 
    The performanced-based approach to leakage rate testing recognizes 
    that historically good results of containment testing provide 
    appropriate assurance of future containment integrity; this supports 
    the conclusion that the impact on the health and safety of the 
    public as a result of extended test intervals is negligible.
        Based on the above, no significant hazards consideration is 
    created by the proposed change.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    Power Station, Unit 2, Shippingport, Pennsylvania
    
        Date of amendment request: March 11, 1996
        Description of amendment request: The proposed amendment would 
    increase the alarm setpoints of the in-containment high range area and 
    containment purge radiation monitors. These alarm setpoints are 
    specified in Table 3.3-6 of Technical Specification 3.3.3.1. The 
    proposed amendment would also include several editorial changes.
        The proposed change to the in-containment high range area radiation 
    monitor alarm setpoint would make the setpoint consistent with the 
    Beaver Valley Power Station Emergency Action Levels (EALs) approved by 
    the NRC in August 1994. These EALs use the in-containment high 
    radiation area monitors as indication of fission product barrier 
    challenges or failures.
        The containment purge radiation monitors are provided to: (1) 
    analyze the ventilation effluent from the reactor containment building, 
    (2) detect abnormal releases and isolate the release if the setpoint is 
    reached or exceeded, and (3) alert refueling personnel of the need to 
    evacuate affected areas so as to maintain occupational exposures as low 
    as reasonably achievable. The proposed increase in this setpoint value 
    provides alarm and isolation based on offsite dose considerations and 
    will provide greater operational flexibility since inadvertent 
    engineered safety feature actuations due to evacuation alarms caused by 
    minor (greater than three times background) increases in radiation 
    levels will be minimized.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed monitor alarm setpoint changes and editorial 
    changes are administrative in nature. Should the in-containment high 
    range area monitors fail to annunciate or give a false alarm, there 
    would be no effect on any other plant equipment or systems. These 
    monitors are safety related; however, they do not initiate any 
    safety function, nor do they interface with any other safety related 
    system. The monitors' alarm as a visual (lighted icon) and audible 
    alarm in the control room. The operator is then responsible for 
    taking any corrective actions necessary, based on the alarm and 
    Emergency Action Level (EAL) guidelines. The in-containment high 
    range area monitors do not provide for any automatic actions of 
    other equipment or systems when an alarm condition occurs.
        The containment purge monitors are also safety related with the 
    ability for an operator to input a radiation level value for high 
    alarm levels during Mode 6, which upon actuation, create both a 
    visual (lighted icon) and
    
    [[Page 15989]]
    audible alarm in the control room. At the high alarm level, each 
    monitor automatically sends a signal to close the purge supply and 
    exhaust isolation dampers in the containment building. A change in 
    the value of the alarm setpoint has no effect on the performance of 
    the containment purge and exhaust system. The high alarm and 
    subsequent automatic termination of a radioactive release will now 
    be based on offsite dose considerations. There is no credible 
    failure of the monitors associated with a change of the alarm 
    setpoint value.
        The operating and design parameters of the subject radiation 
    monitors will not change. The proposed change affects only 
    theradiation level at which an alarm condition is created and does 
    not affect any accident assumptions. The in-containment high range 
    area monitors' alarm setpoint change will not affect the 
    radiological consequences of an accident. However, since the 
    containment purge monitors revised setpoint is based on offsite 
    doses consequences and is a higher value than the current setpoint 
    of three times the background radiation level, the postulated 
    offsite radiological consequences of a fuel handling accident inside 
    containment would be increased. An analysis of a fuel handling 
    accident inside containment with the purge and exhaust system 
    discharging through the Supplementary Leak Collection and Release 
    System (SLCRS) filter trains was performed and a summary of this 
    analysis is to be added to Chapter 15 of the Updated Final Safety 
    Analysis Report (UFSAR). The analysis which determined the 
    containment purge monitors' setpoint postulated offsite doses that 
    are less than a small fraction (less than twenty-five percent) of 
    the 10 CFR Part 100 guidelines. The fuel handling accident inside 
    containment calculation demonstrated control room operator doses 
    that comply with General Design Criteria (GDC) 19. Therefore, the 
    increased radiological consequences of the change in the alarm 
    setpoint are acceptable. The analysis assumed no isolation, so 
    isolation actuated by the monitor alarm will reduce doses further.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed radiation monitor alarm revisions cannot initiate a 
    new type of accident. The referenced radiation monitors' alarms 
    cannot initiate a new type of accident, since even a failure of the 
    monitor itself cannot serve as the initiating event of an accident. 
    Operator action is not made solely on a radiation monitor alarm; 
    other plant condition indicators are also evaluated.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The in-containment high range area monitors have no capability 
    to mitigate the consequences of an accident and do not interface 
    with any safety related system. These monitors are safety related 
    channels which provide indication to the operator of the integrity 
    of the fission product barriers incontainment. This indication, 
    combined with other indications of plant conditions may direct an 
    operator to take action to mitigate the consequences of an accident. 
    The alarm setpoint itself does not perform any specific safety 
    related function and the trip value is not referenced in the UFSAR, 
    nor does any site design basis document take credit for this 
    setpoint. Safety limits and limiting safety system settings are not 
    affected by this proposed change. The site will continue to meet the 
    requirements of 10 CFR Part 100 which limits offsite dose following 
    a postulated fission product release.
        The containment purge monitors' revised setpoint is based on 
    offsite dose consequences and is a higher value than the current 
    setpoint of three times the background radiation level. Thus the 
    postulated offsite radiological consequences of a fuel handling 
    accident inside containment are increased which reduces the current 
    margin of safety. An analysis of a fuel handling accident inside 
    containment with the purge and exhaust system discharging through 
    the SLCRS filter trains was performed and a summary of this analysis 
    will be added to Chapter 15 of the UFSAR. The analysis postulated 
    offsite doses to be less than twenty-five percent of the 10 CFR Part 
    100 guidelines and control room operator doses that comply with GDC 
    19. The analysis shows that the increased radiological consequences 
    of the change in the alarm setpoint are acceptable. Further, the 
    analysis assumed that no isolation would occur; therefore, isolation 
    actuated by the monitors' alarm will reduce the postulated doses.
        Therefore, use of the proposed technical specification would not 
    involve a significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 1500l.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: March 5, 1996
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications (TS) as follows:
        (1) TS Surveillance Requirement (SR) 4.4.3.3: Delete the 
    requirement for testing the switching capability for pressurizer heater 
    power supplies on an 18-month interval.
        (2) TS SR 4.5.2.d: Change the containment sump inspection 
    requirements from each containment entry to once daily if a containment 
    entry has been made and upon the final entry prior to establishing 
    CONTAINMENT INTEGRITY.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
    
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed amendments conform to the uidance given in 
    Enclosure 1 of the NRC Generic Letter 93-05. The overall functional 
    capabilities of the pressurizer heater system and the Emergency Core 
    Cooling System (ECCS) will not be modified by the proposed changes. 
    These amendments will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated for 
    the following reasons:
        (1) Deleting the requirement to test the switching capabilities 
    of the pressurizer heater emergency power supplies will reduce an 
    unnecessary testing requirement since the pressurizer heaters are 
    already connected to the emergency bus.
        (2) Increasing the interval of containment sump inspections to 
    once daily if containment has been entered and upon final entry will 
    reduce unnecessary personnel exposure from performance of 
    containment sump inspections for each containment entry.
        [The staff notes that although statement (2) is correct, it does 
    not provide a reason why the amendments will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated. The staff finds that once daily 
    inspection of the containment adequately ensures that the 
    containment sump remains free of debris.]
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The use of the proposed changes to the TS can not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated since the proposed amendments will not change 
    the physical plant or the modes of plant operation defined
    
    [[Page 15990]]
    in the facility operating license. No new failure mode is introduced 
    due to the surveillance changes and inspection requirements, since 
    the proposed changes do not involve the addition or modification of 
    equipment nor do they alter the design or operation of affected 
    plant systems.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The operating limits and functional capabilities of the affected 
    systems are unchanged by the proposed amendments. The proposed 
    changes to the TS which establish new or clarify old surveillance 
    and inspection requirements [are] consistent with the NRC Generic 
    Letter 93-05 line-item improvement guidance [and] do not 
    significantly reduce any of the margins of safety even though the 
    number of surveillances is decreased. These requested amendments are 
    justified by the following reasoning from NUREG-1366:
        (1) The surveillance or inspection results in radiation exposure 
    to plant personnel which is not justified by the safety significance 
    of the surveillances as in the case of the containment sump 
    inspection requirements.
        (2) The surveillance places an unnecessary burden on plant 
    personnel because the time required is not justified by the safety 
    significance of the surveillance as in the emergency power switching 
    requirements for the pressurizer heater system.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: Eugene V. Imbro
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of amendment requests: February 22, 1996 (AEP:NRC:1243)
        Description of amendment requests: The proposed amendments would 
    revise the technical specifications to reference NRC Regulatory Guide 
    1.9, Revision 3 rather than NRC Regulatory Guide 1.108, Revision 1 
    criteria for the determination of a valid diesel generator test.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Per 10 CFR 50.92, proposed changes do not involve a significant 
    hazards consideration if the changes do not:
        1. involve a significant increase in the probability [or] 
    consequences of an accident previously evaluated,
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. involve a significant reduction in a margin of safety
        Criterion 1
        This amendment request does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because the proposed change to the T/S [technical 
    specifications] does not affect the assumptions, parameters, or 
    results of any UFSAR [updated final safety analysis report] accident 
    analysis.
        The proposed amendment does not modify any existing equipment, 
    and the proposed acceptance criteria for diesel generator testing 
    will conform to NRC guidance. Based on these considerations, it is 
    concluded that the changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Criterion 2
        The proposed changes do not involve physical changes to the 
    plant or changes in plant operating configuration. The proposed 
    changes update guidance for diesel generator testing. Thus, it is 
    concluded that the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        Criterion 3
        The proposed changes update guidance for the testing of diesel 
    generators. The guidance is endorsed by the NRC in Regulatory Guide 
    1.9, and compliance with this guidance will ensure the operability 
    of the diesel generators. Thus, there is no significant reduction in 
    the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Mark Reinhart, Acting
    
    Northeast Nuclear Energy Company (NNECO), Docket No. 50-245, 
    Millstone Nuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of amendment request: December 7, 1995
        Description of amendment request: The proposed change will remove 
    the requirement that primary containment always be purged or vented 
    through the standby gas treatment (SBGT) system and adds requirements 
    that would limit the use of SBGT for purging and venting. The proposed 
    amendment also makes editorial changes and revises the associated Bases 
    section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        NNECO has reviewed the proposed change in accordance with 
    10CFR50.92 and concluded that the change does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    compromised. The proposed change does not involve an SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The proposed change will allow primary containment to be purged 
    or vented without the use of the SBGT system. This change only 
    modifies the alignment of the atmospheric control system for purging 
    or venting containment. The change does not affect any primary 
    system, nor does it affect the ability of the containment isolation 
    valves to close. As such, the proposed change can not affect the 
    probability of occurrence of an accident previously analyzed. This 
    change increases the possibility that some initial post-accident 
    containment atmosphere could be released directly to the atmosphere 
    at the top of the 375 foot stack prior to the closure of the 
    containment isolation valves. However, this condition is bounded by 
    the original radiological release analysis. This is balanced by the 
    increased likelihood that post-accident reactor building atmosphere 
    (from the time that the containment isolation valves close) is 
    processed by the SBGT system.
        The proposed technical specification also establishes strict 
    controls for the use of the SBGT system for purging and venting 
    containment atmosphere. This includes disabling the automatic 
    initiation of the train not in use and relying on a dedicated 
    operator to initiate the remaining train, should a DBA [design basis 
    accident] occur. Since SBGT system operation does not affect the 
    initiation of any postulated accident, disabling the automatic 
    initiation and relying upon operator action to start the remaining 
    train can not affect the probability of an accident previously 
    evaluated. The failure of the train to start within one minute 
    following the DBA could increase the consequences of
    
    [[Page 15991]]
    an analyzed accident. To ensure timely initiation, NNECO has 
    implemented a procedure for purging or venting through the SBGT 
    system which establishes a dedicated operator whose function at the 
    onset of a DBA is to isolate the train in use (the train expected to 
    be damaged by the pressure spike), verify the open AC [atmospheric 
    control] valves go closed, and then start the second train. This 
    procedure has been validated to ensure that these actions can be 
    completed within one minute.
        Although not expected, a delay in operator action to initiate 
    the SBGT has been evaluated for impact upon the radiological 
    consequences. The evaluation shows that the offsite doses remain 
    well within the 10CFR100 limit even if the operator actions are not 
    completed until three minutes after the DBA occurs.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed change allows removal of the SBGT system from the 
    release path for normal containment purge and venting. The change 
    does not affect the frequency or requirement for venting. Nor does 
    the proposed LCO [limiting condition for operation] affect the 
    processes of venting or purging primary containment; the same 
    penetrations and containment isolation valves will continue to be 
    used. All purging and venting functions can still be performed when 
    required by existing specifications and plant procedures. The 
    proposed change does not diminish the capability of any isolation 
    valve for performing its isolation function.
        Therefore, the proposed change can not create a new or different 
    kind of accident.
        3. Involve a significant reduction in the margin of safety.
        The affect of this change has been analyzed against the criteria 
    of 10CFR100 and 10CFR20. The potential release which may occur as a 
    result of a postulated DBA while purging or venting directly to the 
    stack will not exceed the limits of 10CFR100. Likewise, the 
    technical specifications and administrative controls established for 
    purging or venting through the SBGT minimize the potential for an 
    unfiltered release should a DBA occur during that evolution. 
    Further, the amount of time that a SBGT train is aligned to primary 
    containment is expected to be substantially reduced from that 
    required by the existing Technical Specification. Decreasing the 
    amount of time that SBGT is aligned to primary containment decreases 
    the possibility that a DBA would occur while in such an alignment.
        Finally, the potential increase in dose which could occur as a 
    result of normal purge and vent activities will be controlled such 
    that it remains below acceptable limits.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: January 17, 1996
        Description of amendment requests: The proposed amendment would 
    revise selected technical specifications (TS) in accordance with the 
    NRC's Final Policy Statement on TS Improvements for Nuclear Power 
    Reactors and relocate the TS to the Diablo Canyon Power Plant Equipment 
    Control Guidelines. The proposed change would also create TS 6.8.4.j, 
    ``Explosive Gas and Storage Tank Radioactivity Monitoring Program.'' 
    Some of the TS would be relocated and maintained in accordance with 
    this program. Specifically, the following TS would be relocated: TS 
    3.1.2.1, ``Boration Systems Flow Path - Shutdown,'' TS 3.1.2.3, 
    ``Charging Pumps - Shutdown,'' TS 3.1.2.4, ``Charging Pumps - 
    Operating,'' TS 3.1.2.5, ``Borated Water Sources - Shutdown,'' TS 
    3.1.2.6, ``Borated Water Sources - Operating,'' TS 3.3.3.2, ``Movable 
    Incore Detectors,'' TS 3.3.3.4, ``Meteorological Instrumentation,'' TS 
    3.3.3.10, ``Explosive Gas Effluent Monitoring Instrumentation,'' TS 
    3.9.3, ``Decay Time,'' TS 3.9.5, ``Communications,'' TS 3.9.6, 
    ``Manipulator Crane,'' TS 3.9.7, ``Crane Travel - Fuel Handling 
    Building,'' TS 3.9.10.2, ``Water Level - Reactor Vessel - Control 
    Rods,'' TS 3.9.13, ``Spent Fuel Shipping Cask Movement,'' TS 3.10.1, 
    ``Special Test Exceptions - Shutdown Margin,'' TS 3.10.4, ``Position 
    Indication System - Shutdown,'' TS 3.11.1.4, ``Liquid Holdup Tanks,'' 
    TS 3.11.2.5, ``Explosive Gas Mixture,'' and TS 3.11.2.6, ``Gas Storage 
    Tanks.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes simplify the Technical Specifications (TS), 
    meet regulatory requirements for relocated TS, and implement the 
    recommendations of the Commission's Final Policy Statement on TS 
    Improvements and revised 10 CFR 50.36. Future changes to these 
    requirements will be controlled by 10 CFR 50.59. The proposed 
    changes are administrative in nature and do not involve any 
    modifications to any plant equipment or affect plant operation.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are administrative in nature, do not 
    involve any physical alterations to any plant equipment, and cause 
    no change in the method by which any safety-related system performs 
    its function. Also, no changes to the operation of the plant or 
    equipment are involved.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes involve relocating TS requirements to a 
    licensee-controlled document. The requirements to be relocated were 
    identified by applying the criteria endorsed in the Commission's 
    Final Policy Statement, which is included in the new revision of 10 
    CFR 50.36, and are consistent with NUREG-1431, Rev. 1. Thus, the 
    proposed changes do not alter the basic regulatory requirements and 
    do not affect any safety analysis.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
        
    [[Page 15992]]
    
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: February 12, 1996
        Description of amendment request: The amendments would revise the 
    Susquehanna Units 1 and 2 Technical Specifications establish and 
    reference a Primary Containment Leakage Rate Testing Program in order 
    to implement 10 CFR 50, Appendix J, Option B in accordance with the 
    guidelines contained in Regulatory Guide 1.163, ``Performance-Based 
    Containment Leak-Test Program'', dated September 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed license amendments do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The proposed license amendments revise the 
    Technical Specifications to reflect the adoption of a performance-
    based containment leakage-testing program. The Nuclear Regulatory 
    Commission has approved the use of a performance-based option for 
    containment leakage testing programs when it amended 10 CFR Part 50, 
    Appendix J (60 FR 49495).
        To adopt of (sic) the revised regulations, licensees are 
    required to incorporate into their Technical Specifications, by 
    general reference, the NRC regulatory guide or other plant specific 
    implementing document. A new Administrative Controls Specification 
    is being added to the Susquehanna SES Technical Specifications that 
    requires the establishment and maintenance of a Primary Containment 
    Leakage Rate Testing Program. As stated in the Technical 
    Specification, this Primary Containment Leakage Rate Testing Program 
    will conform with NRC Regulatory Guide 1.163, ``Performance-Based 
    Containment Leak-Rate Testing Program'', dated September 1995. The 
    Primary Containment Leakage Rate Testing Program establishes 
    requirements intended to ensure on-going containment integrity, 
    including the performance of a periodic general visual inspection of 
    the containment to detect early indications of structural 
    deterioration.
        The effect of increasing containment leakage rate testing 
    intervals has been evaluated by the Nuclear Energy Institute using 
    the methodology described in NUREG-1493 and historical 
    representative industry leakage rate testing data. The results of 
    this evaluation, as published in NEI 94-01, Revision 0, are that the 
    increased risk corresponding to the extended test interval is small 
    (less than 0.1 percent of total risk) and compares well to the 
    guidance of the NRC's safety goal. The primary containment leak rate 
    data and component performance history at Susquehanna SES are 
    consistent with the conclusions reached in NUREG-1493 and NEI 94-01. 
    Therefore, adoption of performance-based verification of leakage 
    rates for isolation valves, containment penetrations, and the 
    overall containment boundary will provide an equivalent level of 
    safety and does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        II. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        No safety-related equipment, safety function, or plant 
    operations will be altered as a result of the proposed license 
    amendment.
        The safety objective for the primary containment is stated in 10 
    CFR 50, Appendix A, ``General Design Criteria for Nuclear Power 
    Plants.'' The safety function of the primary containment will be met 
    since the containment will continue to provide ``an essentially leak 
    tight barrier against the uncontrolled release of radioactivity to 
    the environment...'' for postulated accidents. Therefore, the 
    proposed license amendments will not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        III. This change does not involve a significant reduction in a 
    margin of safety.
        As stated above, the Nuclear Regulatory Commission has approved 
    the use of a performance-based option for containment leakage 
    testing programs when it amended 10 CFR Part 50, Appendix J (60 FR 
    49495). The new Primary Containment Leakage Rate Testing Program 
    will conform with NRC Regulatory Guide 1.163, Revision 0, dated 
    September 1995, ``Performance-Based Containment Leak-Rate Testing 
    Program'' by requiring that leakage testing intervals be established 
    based on the criteria in Section 11.0 of NEI 94-01, Revision 0.
        As discussed in Part 1 above, the effect of increasing 
    containment leakage rate testing intervals has been evaluated by the 
    Nuclear Energy Institute using the methodology described in NUREG-
    1493 and historical representative industry leakage rate testing 
    data. The results of this evaluation, as published in NEI 94-01, 
    Revision 0, are that the increased safety risk corresponding to the 
    extended test intervals is small (less than 0.1 percent of total 
    risk) and compares well to the guidance of the NRC's safety goal. In 
    addition, as demonstrated by risk analyses contained in NUREG-1482, 
    relaxation of the integrated leak rate test frequency does not 
    significantly increase the probability or consequences of a 
    previously evaluated accident. Integrated leakage rate tests have 
    been demonstrated to be of limited value in detecting significant 
    leakages from penetrations and isolation valves. The primary 
    containment leak rate data and component performance history at 
    Susquehanna SES are consistent with the conclusions reached in 
    NUREG-1493 and NEI 94-01. Therefore, the proposed license amendments 
    adopting a performance-based approach for verification of leakage 
    rates for isolation valves, containment penetrations, and the 
    containment overall will continue to meet the regulatory goal of 
    providing an essentially leak-tight containment boundary, will 
    provide an equivalent level of safety, and do not involve a 
    significant reduction in a margin of safety.
        The revised Technical Specifications will continue to maintain 
    the allowable leak rate (La) as the Type A test performance 
    criterion. In addition, a requirement to perform a periodic general 
    visual inspection of the containment is part of the performance-
    based leakage testing program.
        The revised Technical Specifications will continue to maintain 
    the allowable leak rate (La) as the Type B and C tests' performance 
    criterion. As supported by the findings of NUREG-1493, the 
    percentage of leakages detected only by integrated leak rate tests 
    is small (only a few percent) and Type B and C leakage tests are 
    capable of detecting more than 97 percent of containment leakages 
    and virtually all such leakages are identified by local leak rate 
    tests (LLRTs) of containment isolation valves.
        Thus, the proposed license amendments do not involve a 
    significant reduction in a margin of safety and will continue to 
    support the regulatory goal of ensuring an essentially leak-tight 
    containment boundary.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: February 23, 1996
        Description of amendment request: The proposed amendment would 
    change the Technical Specification (TS) Surveillance Requirement 
    4.6.2.1d concerning drywell-to suppression chamber bypass testing. 
    Currently, Susquehanna TSs require the performance of a bypass test at 
    40 plus or minus 10-month intervals. The proposed TS change would 
    request that the bypass test interval be revised to correspond with the 
    interval for Primary Containment Integrated Leak Rate
    
    [[Page 15993]]
    Testing (ILRT) under 10 CFR Part 50, Appendix J, Option B.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change to allow bypass testing at the [Integrated 
    Leak Rate Testing] interval involves no physical or operational 
    changes to the Susquehanna SES. Reviews of bypass leakage test 
    results at Susquehanna and other similarly designed plants confirm 
    that minimal suppression pool bypass leakage has occurred. Based on 
    this data, the risk of suppression pool bypass leakage from non 
    vacuum breaker sources is no greater than that of other primary 
    containment passive structures which are tested at the ILRT 
    frequency. Leak testing of the drywell-to-suppression chamber vacuum 
    breakers will continue to be performed on a refueling and inspection 
    outage frequency to ensure that their contribution to the leakage 
    area is acceptable. In addition, inspection of the diaphragm slab 
    within the testing interval provides additional assurance that any 
    degradation to the structure will be detected and resolved. 
    Therefore, the pressure suppression capability of the containment is 
    not reduced from the existing design, and there will be no 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        II. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change to allow bypass testing at the ILRT interval 
    involves no physical or operational changes to the Susquehanna SES. 
    The surveillance change does not impact the LOCA response of the 
    units, or impact the design basis of the units in any way. 
    Therefore, the possibility of a new or different kind of accident 
    will not be created.
        III. This change does not result in a significant reduction in a 
    margin of safety.
        The drywell-to-suppression chamber bypass leak test data 
    obtained during previous testing at Susquehanna SES and other 
    similarly designed plants demonstrates conformance, by a large 
    margin, to the Technical Specification and design leakage 
    requirements. The test data and safety analysis provided here 
    indicate that there is negligible risk that the bypass leakage will 
    change adversely in future years. Furthermore, the proposed 
    performance based test methodology is judged to be acceptable based 
    on the small risk of bypass leakage through paths other than those 
    containing the suppression pool vacuum breakers. Testing of the 
    bypass leak pathway containing the vacuum breakers will be used to 
    verify acceptable bypass leakage during those outages when the 
    bypass leak test is not performed. In addition, periodic visual 
    inspection of the diaphragm slab within the bypass test interval 
    provides additional assurance that any degradation to the structure 
    will be detected and resolved.
        Testing of the bypass leakage pathways containing vacuum 
    breakers, with stringent acceptance criteria, combined with the 
    other negligible potential leakage areas, and periodic inspection of 
    the diaphragm slab, provide an acceptable level of assurance that 
    the bypass leakage will be minimized. The proposed performance based 
    approach to bypass testing and inspection ensures that adverse 
    conditions can be detected and corrected such that the existing 
    level of confidence that the primary containment will function as 
    required during a LOCA is maintained. Therefore, the proposed 
    Technical Specification changes do not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: February 29, 1996
        Description of amendment request: The proposed amendment relocates 
    Technical Specification 3/4.9.6, ``Refueling Platform,'' to the 
    Technical Requirements Manual, which is controlled under the 
    requirements of 10 CFR 50.59.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involves a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change relocates the provisions of the Refueling 
    Platform that are contained in the Technical Specifications and 
    places them in the Technical Requirements Manual. Review and 
    approval of those portions of the Refueling Platform requirements 
    contained in the Technical Requirements Manual and revisions thereto 
    will be the responsibility of the Plant Operations Review Committee 
    just as it was their responsibility to review changes to the 
    refueling platform Limiting Condition for Operation and Surveillance 
    Requirements when they were part of the Technical Specifications. 
    Requiring review by the Plant Operations Review Committee reinforces 
    the importance of the Technical Requirements manual and the 
    requirements controlled by it and assures a multidisciplined review. 
    Approved Technical Requirements or changes thereto are provided to 
    the Susquehanna Review Committee for information. No design basis 
    accidents are affected by the change, nor are safety systems 
    adversely affected by the change. Therefore, these changes will not 
    result in any change to current Technical Specification 
    requirements, but will reduce the level of regulatory control 
    associated with the identified requirements. The level regulatory 
    control has no impact on the probability or the consequences of an 
    accident previously evaluated, therefore, the proposed change will 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed change relocates the provisions of the Refueling 
    Platform that are contained in the Technical Specifications and 
    places them in the Technical Requirements Manual. This change will 
    not involve any physical changes to the Refueling Platform and its 
    associated instrumentation nor any changes in the manner in which 
    this equipment is operated, maintained, tested or inspected. Future 
    changes to these relocated requirements or surveillances will be 
    evaluated in accordance with the requirements of 10CFR50.59. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The margin of safety is not reduced. The relocated requirements 
    do not meet any of the four criteria in the NRC Policy Statement 
    used for defining the scope of Technical Specifications. In 
    addition, the relocated requirements and surveillances for the 
    refuel platform and associated instrumentation remain the same as 
    stated in the existing Technical Specifications. Future changes to 
    these relocated requirements or surveillances will be evaluated in 
    accordance with the requirements of 10CFR50.59. Review and approval 
    of those portions of the Refueling Platform requirements contained 
    in the Technical Requirements Manual and the revisions thereto will 
    be the responsibility of the Plant Operations Review Committee just 
    as it was their responsibility to review changes to the refueling 
    platform Limiting Condition for Operation and Surveillance 
    Requirements when they were part of the Technical Specifications. 
    Approved Technical Requirements or changes thereto are provided to 
    the Susquehanna Review Committee for information. Therefore, no
    
    [[Page 15994]]
    significant reduction in a margin to safety is proposed.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: February 29, 1996
        Description of amendment request: The proposed amendment removes 
    the Rod Block Monitor (RBM) requirements from the Technical 
    Specifications, thereby reducing the number of rod movements during 
    power maneuvers.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change removes the Rod Block Monitor requirements 
    from Technical Specifications based on no credit being taken for the 
    RBM in the reload licensing analysis. The RBM was originally 
    designed to prevent fuel damage during the Rod Withdrawal Error 
    [RWE] event by automatically stopping control rod motion before any 
    fuel design limits are exceeded. However, due to control rod drift 
    events in which the RBM can not (sic) stop control rod motion, the 
    RWE is analyzed without taking credit for the RBM. The results of 
    this analysis are operating limits that prevent fuel damage from a 
    RWE in which control rod motion is not stopped by the RBM. 
    Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        This proposed change of removing the RBM requirements from 
    Technical Specifications does not change the currently approved 
    approach for performing the reload licensing analysis for either 
    Unit. To date all reload analyses have been performed considering 
    the rod drift event as a moderate frequency event and no credit 
    being taken for the RBM. Since no credit is taken, removal of these 
    requirements from Technical Specifications does not impact the 
    current approach for performing reload analysis. Therefore, this 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        Continued compliance to the governing General Design Criteria 
    [GDC] for the RWE analysis assumes an appropriate margin of safety.
        GDC 10 is met when the specified acceptable fuel design limits 
    (SAFDLs) are not exceeded for the RWE. The first SAFDL requires that 
    a MCPR [Minimum Critical Power Ratio] Operating Limit be determined 
    such that the reduction of MCPR margin due to an RWE does not 
    violate the MCPR Safety Limit. The second SAFDL requires that the 
    uniform cladding strain does not exceed 1% during an RWE. PP&L's 
    [Pennsylvania Power and Light Company] licensing analysis of the 
    RWE, without taking credit for the RBM, determines a MCPR Operating 
    limit such that the reduction of MCPR margin due to an RWE does not 
    violate the MCPR Safety Limit and validates that the maximum uniform 
    cladding strain is less than 1%. Therefore, the applicable SAFDLs 
    for the RWE are satisfied and the GDC requirements met.
        GDC 20 is met when the reactivity control system is 
    automatically actuated to prevent exceeding the SAFDLs. PP&L's 
    licensing analysis of the RWE, without taking credit for the RBM, 
    conservatively determines a MCPR Operating Limit and validates that 
    the maximum uniform cladding strain is less than 1%. Therefore, 
    actuation of the RBM is not necessary to prevent exceeding the 
    applicable SAFDLs for the RWE.
        GDC 25 is met when a single malfunction in the reactivity 
    control system will not cause the SAFDLs to be exceeded. The current 
    RWE licensing analysis assumes a control rod drift event without any 
    credit for the RBM. With respect to the reactivity control system, 
    the assumptions of a control rod drift event and no actuation of the 
    RBM are more conservative than the assumptions in the original SSES 
    Safety Evaluation. Therefore, the requirements from GDC 25 are still 
    met. Therefore, no significant reduction in the safety margin 
    exists.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: February 9, 1996, as supplemented March 
    15, 1996. This notice supersedes the notice published on February 28, 
    1996 (61 FR 7557) in its entirety.
        Description of amendment request: The proposed amendment would 
    revise the Administrative Controls Section 5.6.6 of the Ginna Technical 
    Specifications (TSs) to incorporate a reference to the methodology for 
    determining pressure/temperature (P/T) and low-temperature overpressure 
    protection (LTOP) limits. The proposed amendment would follow guidance 
    given in Generic Letter 96-03 for relocating LTOP and the reactor 
    coolant system (RCS) P/T limits to the RCS Pressure and Temperature 
    Limits Report (PTLR). The proposed amendment will allow the licensee to 
    perform future LTOP and RCS P/T evaluations, using NRC-approved 
    methodology, without requiring changes to the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated. The proposed 
    changes only require that future RCS P/T and LTOP limits be 
    developed using NRC approved methodology as specified within the 
    Administrative Controls section and do not involve any technical 
    changes. As such, these changes are administrative in nature and do 
    not impact initiators or analyzed events or assumed mitigation of 
    accident or transient events. Therefore, these changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously analyzed.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The proposed 
    changes do not involve a physical alteration of the plant (i.e., no 
    new or different type of equipment will be installed) or changes in 
    the methods governing normal plant operation. The proposed changes 
    will not impose any new or different requirements. Thus, this change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
    
    [[Page 15995]]
    
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety. The proposed changes will not reduce a margin of plant 
    safety because the changes do not impact any safety analysis 
    assumptions other than requiring future evaluations of RCS P/T and 
    LTOP limits to be performed in accordance with NRC approved 
    methodology. These changes are administrative in nature. As such, no 
    question of safety is involved, and the change does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005 NRC Acting Project Director: Susan 
    Frant Shankman
    
    South Carolina Electric & Gas Company (SCE&G), South Carolina 
    Public Service Authority, Docket No. 50-395, Virgil C. Summer 
    Nuclear Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: March 19, 1996
        Description of amendment request: The licensee is proposing to 
    change the Technical Specification (TS) 3/4.2.4, QUADRANT POWER TILT 
    RATIO (QPTR), the Bases for QPTR, and TS 3/4.3.1, REACTOR TRIP SYSTEM 
    INSTRUMENTATION, Table 3.3-1, ``Table Notation, Action Statement 2.c.'' 
    The licensee is requesting the changes in order to use the guidance in 
    the improved Westinghouse Standardized Technical Specifications, NUREG 
    1431, Rev. 1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The probability or consequences of an accident previously 
    evaluated in the FSAR is not significantly increased.
        The QPTR limits ensure that FNdelta-H and FQ(z) 
    remain below their limiting values by preventing an undetected 
    change in the gross radial power distribution. In MODE 1, the 
    FNdelta-H and FQ(z) limits must be maintained to 
    preclude core power distributions from exceeding design limits 
    assumed in the safety analyses. The QPTR satisfies Criterion 2 of 
    the NRC Policy Statement.
        The QPTR limit of 1.02, at which corrective action is required, 
    provides a margin of protection for both the departure from nucleate 
    boiling ratio and linear heat generation rate contributing to 
    excessive power peaks resulting from X-Y plane power tilts. A 
    limiting QPTR of 1.02 can be tolerated before the margin for 
    uncertainty in FQ(z) and FNdelta-H is possibly 
    challenged. With the QPTR exceeding its limit, a power level 
    reduction of 3% from RATED THERMAL POWER for each 1% by which the 
    QPTR exceeds 1.00 is a conservative tradeoff of total core power 
    with peak linear power.
        The Power Range Neutron Flux trip setpoint reduction is not 
    required since incore flux measurements are not expected to change 
    concurrent with the loss of a Power Range Channel. These setpoints, 
    which were previously reduced in order to account for uncertainties, 
    will now be monitored and corrected, if necessary, per TS 3.2.4.
        Any change in the QPTR would be detected by requiring a check of 
    the QPTR once per 12 hours. If the QPTR indicates an increase, 
    THERMAL POWER has to be reduced accordingly. A 12 hour completion 
    time is sufficient because any additional change in QPTR would be 
    relatively slow.
        The improvement of TS 3/4.2.4 to reflect the improved STS in no 
    way impacts the accident analysis of the FSAR. Therefore, the 
    probability or consequences of a previously evaluated accident has 
    not been increased.
        2. The possibility of an accident or a malfunction of a 
    different type than any previously evaluated is not created.
        The proposed amendment request does not necessitate physical 
    alteration of the plant nor changes in parameters governing normal 
    plant operation. Therefore, the change does not create the 
    possibility of a new or different kind of accident or malfunction.
        3. The margin of safety has not been significantly reduced.
        This proposed amendment request precludes core power 
    distributions that may lead to violation of the following fuel 
    design criteria:
        a. During a large break loss of coolant accident, the peak 
    cladding temperature must not exceed 2200 deg.
        b. During a loss of forced reactor coolant flow accident, there 
    must be at least 95% probability at the 95% confidence level (the 
    95/95 departure from nucleate boiling (DNB) criterion) that the hot 
    fuel rod in the core does not experience a DNB condition;
        c. During an ejected rod accident, the energy deposition to the 
    fuel must not exceed 280 cal/gm; and
        d. The control rods must be capable of shutting down the reactor 
    with a minimum required shutdown margin with the highest worth 
    control rod stuck fully withdrawn.
        The improvement of TS 3/4.2.4 ensures that the gross radial 
    power distribution remains consistent with the design values used in 
    the safety analyses.
        The core peaking factors and the quadrant tilt must be evaluated 
    because they are the factors that best characterize the core power 
    distribution. This reevaluation is required to ensure that the 
    reactor core conditions are consistent with the assumptions in the 
    safety analyses. Therefore, the margin of safety has not decreased.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: Frederick J. Hebdon
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: November 2, 1995
        Description of amendment requests: The licensee proposes to revise 
    Technical Specification (TS) 3.8.1, ``AC Sources - Operating,'' of the 
    improved TS, to (1) extend the offsite circuit allowed outage time 
    (AOT) from ``72 hours AND 6 days from discovery of failure to meet 
    LCO'' to ``72 hours AND 10 days from discovery of failure to meet LCO'' 
    and (2) extend the emergency diesel generator (EDG) AOT from ``72 hours 
    AND 6 days from discovery of failure to meet LCO'' to ``7 days AND 10 
    days from discovery of failure to meet LCO.'' Additionally, the 
    licensee proposes to further extend the EDG AOT to ``10 days AND 10 
    days from discovery of failure to meet LCO'' on a once-per-refueling 
    cycle frequency for maintenance purposes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Emergency Diesel Generators (EDGs) are backup alternating 
    current power sources designed to power essential safety systems in 
    the event of a loss of offsite power. EDGs are not accident 
    initiators in any accident previously evaluated. Therefore, this 
    change does not involve an increase in the probability of an 
    accident previously evaluated.
        The EDGs provide backup power to components that mitigate the 
    consequences of accidents. The proposed changes to the Allowed 
    Outage Times (AOTs) do not affect
    
    [[Page 15996]]
    any of the assumptions used in the deterministic safety analysis.
        To fully evaluate the effect of the EDG AOT extension, 
    Probabilistic Safety Analysis (PSA) methods were utilized. The 
    results of these analyses show no significant increase in the core 
    damage frequency. As a result, there would be no significant 
    increase in the consequences of accidents previously evaluated.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This proposed change does not alter the design, configuration, 
    or method of operation of the plant. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect the Limiting Conditions for 
    Operation or their Bases that are used in the deterministic analyses 
    to establish the margin of safety. PSA evaluations were used to 
    evaluate these changes, and these evaluations determined that the 
    changes are either risk neutral or risk beneficial.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P.O. Box 800, Rosemead, California 91770
        NRC Project Director: William H. Bateman
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: November 6, 1995
        Description of amendment requests: The licensee proposes to revise 
    Technical Specification (TS) 3.5.1, ``Safety Injection Tanks (SITs),'' 
    of the improved TS to extend, in general, the allowed outage time (AOT) 
    for a single inoperable SIT from 1 hour to 24 hours. Additionally, the 
    licensee proposes to extend the SIT AOT from 1 hour to 72 hours if a 
    single SIT becomes inoperable due to malfunctioning SIT water level 
    and/or nitrogen cover pressure instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Safety Injection Tanks (SITs) are passive components in the 
    Emergency Core Cooling System (ECCS). The SITs are not accident 
    initiators in any accident previously evaluated.
        Therefore, this change does not involve an increase in the 
    probability of an accident previously evaluated.
        The SITs are designed to mitigate the consequences of Loss of 
    Coolant Accidents (LOCAs). The proposed changes do not affect any of 
    the assumptions used in deterministic LOCA analysis. Therefore, the 
    consequences of accidents previously evaluated do not change.
        To fully evaluate the SIT Allowed Outage Time (AOT) extension, 
    Probabilistic Safety Analysis (PSA) methods were utilized. The 
    results of these analyses show no significant increase in core 
    damage frequency. As a result, there would be no significant 
    increase in the consequences of an accident previously evaluated.
        The proposed change pertaining to SIT inoperability based solely 
    on instrumentation malfunction does not involve a significant 
    increase in the consequences of an accident as evaluated and 
    endorsed by the Nuclear Regulatory Commission (NRC) in NUREG-1366, 
    ``Improvements to Technical Specifications Surveillance 
    Requirements.''
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This proposed change does not change the design, configuration, 
    or method of operation of the plant. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes do not affect the limiting conditions for 
    operation or their bases that are used in the deterministic analyses 
    to establish the margin of safety. PSA evaluations were used to 
    evaluate these changes. These evaluations demonstrate that the 
    changes are either risk neutral or risk beneficial.
        Therefore, this change does not involve a significant reduction 
    in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770
        NRC Project Director: William H. Bateman
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: November 8, 1995
        Description of amendment requests: The licensee proposes to revise 
    Technical Specification (TS) 3.5.2, ``ECCS - Operating,'' in the 
    improved TS to extend the allowed outage time from 72 hours to 7 days 
    for a single low pressure safety injection (LPSI) train.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Low Pressure Safety Injection (LPSI) system is a part of the 
    Emergency Core Cooling System (ECCS). Inoperable LPSI components are 
    not considered to be accident initiators. Therefore, this change 
    does not involve an increase in the probability of an accident 
    previously evaluated.
        The LPSI system is primarily designed to mitigate the 
    consequences of a large Loss of Coolant Accident (LOCA). This 
    proposed change does not affect any of the assumptions used in the 
    deterministic LOCA analysis. Therefore, the consequences of 
    accidents previously evaluated do not change.
        To fully evaluate the LPSI Allowed Outage Time (AOT) extension, 
    Probabilistic Safety Analysis (PSA) methods were utilized. The 
    results of these analyses show no significant increase in core 
    damage frequency. As a result, there would be no significant 
    increase in the consequences of an accident previously evaluated.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
    
    [[Page 15997]]
    
        This proposed change does not change the design, configuration, 
    or method of operation of the plant. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not affect the limiting conditions for 
    operation or their bases that are used in the deterministic analyses 
    to establish the margin of safety. PSA evaluations were used to 
    evaluate these changes.
        Therefore, this change does not involve a significant reduction 
    in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770
        NRC Project Director: William H. Bateman
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: December 6, 1995
        Description of amendment requests: The licensee proposes to revise 
    Technical Specification (TS) 4.3, ``Fuel Storage,'' of the improved TS, 
    to allow fuel assemblies having a maximum U-235 enrichment of 4.8 
    weight percent to be stored in both the spent fuel racks and the new 
    fuel racks.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        There is no increase in the probability of an accident because 
    the physical characteristics of a fuel assembly are not changed when 
    fuel enrichment is increased. No changes will be made to any safety 
    related equipment or systems. Fuel assembly movement will continue 
    to be controlled by approved fuel handling procedures.
        Fuel cycle designs will continue to be analyzed with Nuclear 
    Regulatory Commission (NRC)-approved codes and methods to ensure the 
    design bases for San Onofre Units 2 and 3 are satisfied.
        The double contingency principle of American National Standards 
    Institute/American Nuclear Society (ANSI/ANS) Standard 8.1-1983 can 
    be applied to any postulated accident in the Spent Fuel Pool (SFP) 
    which could cause reactivity to increase. In conjunction with 
    administrative controls for heavy loads and impact zones, a boron 
    concentration of 1850 parts per million (PPM) (the current Technical 
    Specification (TS) limit) is sufficient to maintain k-eff less than 
    or equal to 0.95 for all normal and postulated accident conditions.
        Regarding the new fuel storage racks, there is no postulated 
    accident which could cause reactivity to increase above 0.95 for all 
    moderator densities from 0.0 to 1.0 grams/cubic centimeter (gms/cc).
        The radiological consequence analyses performed in the Updated 
    Final Safety Analysis Report (UFSAR) include the development of 
    source terms which bound discharge fuel burnups to 60,000 megawatt 
    days per ton (MWD/T). Increasing the San Onofre Units 2 and 3 
    enrichment to 4.8 weight percent (w/o) does not result in discharge 
    fuel assembly burnups greater than 60,000 MWD/T. Thus, the 
    consequences of the fuel handling accident are unchanged from the 
    current UFSAR bases.
        Therefore, this proposed change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not involve any physical changes to the 
    plant or any changes to the method in which the plant is operated. 
    They do not affect the performance or qualification of safety 
    related equipment. Fuel handling accidents were previously 
    considered. Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated is not created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        For the SFP, the NRC acceptance criteria is k-eff less than or 
    equal to 0.95 under all normal and accident conditions and including 
    uncertainties. For the new fuel storage racks, k-eff must remain 
    less than 0.95 if completely flooded with unborated water, and must 
    remain below 0.98 in an optimum moderation event. Analyses have been 
    performed which demonstrate that these acceptance criteria will 
    continue to be met when the enrichment is increased to 4.8 w/o.
        The current UFSAR design bases SFP decay heat loads bound the 
    proposed enrichment increase due to the reduced fuel batch size.
        Radiological effects of fuel handling accidents are unchanged by 
    this enrichment increase.
        The proposed design of the higher enriched fuel will result in a 
    slight weight increase. However, the seismic event is bounded by the 
    analyses performed for the rerack project.
        Therefore, there will not be a significant reduction in a margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770
        NRC Project Director: William H. Bateman
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: January 4, 1996
        Description of amendment requests: The licensee proposes to delete 
    License Conditions 2.C(26) and 2.C(27). These license conditions 
    require the licensee to implement and maintain a plan for scheduling 
    all capital modifications based on an NRC approved Integrated 
    Implementation Schedule Program Plan.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change deletes an administrative means of tracking 
    and scheduling NRC required plant modifications and license 
    commitments. It does not affect the plant configuration nor NRC 
    mandated schedules for implementation of modifications. Because the 
    deletion of the license condition does not affect the plant 
    configuration, no accident analyses are affected; therefore, the 
    proposed change does not increase the probability or consequences of 
    any previously evaluated accident.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change will not alter the configuration of the 
    plant or its operation; therefore, the proposed change does not 
    create a new or different kind of accident from any previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change is administrative and does not affect any 
    accident analyses or
    
    [[Page 15998]]
    involve any modification to the plant configuration; therefore, the 
    proposed change does not involve a reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, California 91770
        NRC Project Director: William H. Bateman
    
    Tennessee Valley Authority, Docket Nos. 50-390 Watts Bar Nuclear 
    Plant, Unit 1, Rhea County, Tennessee
    
        Date of amendment request: February 28, 1996
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) to extend the ice weighing and 
    flow channel inspection surveillance frequencies from 9 to 18 months. 
    Concurrently, the required total ice bed weight would be increased from 
    2,360,875 to 2,403,800 lbs. to account for the anticipated additional 
    ice sublimation during the longer interval between weighing and 
    inspection.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's analysis is 
    presented below.
        1. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The ice condenser system is provided to absorb thermal energy 
    release following a LOCA or high energy line break (HELB) and to limit 
    the peak pressure inside containment. The containment analysis for 
    Watts Bar is based on a minimum of 1093 lbs of ice per ice basket 
    evenly distributed throughout the ice condenser, and the subcompartment 
    analysis is based on 85 percent of the available flow area (flow 
    channels) being open uniformly throughout the ice condenser. For the 
    predicted sublimation rate of up to 12 percent for 18 months, an 
    average ice basket weight of 1093 lbs at the end of the 18 month period 
    would still be available. An evaluation of the operating history of the 
    other operating ice condenser plants shows that after 18 months 85 
    percent of the flow channels will still be available.
        Thus the ice condenser will perform its design functions with the 
    revised minimum ice weight and inspection interval. There will be no 
    design change or other operational changes. Accordingly, the proposed 
    changes to the technical specifications do not affect the probability 
    or consequences of an accident.
        2.
        The changes do not create the possibility of a new or different 
    kind of accident from any previously analyzed.
        As stated above, the proposed changes do not involve modifications 
    to the ice condenser or other plant systems. Hence there is no 
    possibility of a new or different kind of accident since no new design 
    is involved.
        3. The changes do not involve a significant reduction in a margin 
    of safety.
        Plant safety margins are established through limiting conditions of 
    operation, limiting safety system settings, and safety limits specified 
    in the TS. None of these will be changed.
        Based on this analysis, it appears that the three standards of 10 
    CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-390 Watts Bar Nuclear 
    Plant,Unit 1, Rhea County, Tennessee
    
        Date of amendment request: February 28, 1996
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) surveillance frequency for 
    Westinghouse type AR relays, used as solid state protection system 
    slave relays or auxiliary relays, from quarterly to a refueling outage 
    frequency.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Operation of the facility in accordance with the proposed
        amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        This change to the Technical Specifications does not result in a 
    condition where the design, material, and construction standards 
    that were applicable prior to the change are altered. The same ESFAS 
    instrumentation is being used and the same ESFAS system reliability 
    is expected. The proposed change will not modify any system 
    interface or function and could not increase the likelihood of an 
    accident since these events are independent of this change. The 
    proposed activity will not change, degrade or prevent the 
    performance of any accident mitigation systems or alter any 
    assumptions previously made in evaluating the radiological 
    consequences of an accident described in the safety analysis report. 
    Therefore, the proposed amendment does not result in any increase in 
    the probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        This change does not alter the performance of the ESFAS 
    mitigation systems assumed in the plant safety analysis. Changing 
    the interval for periodically verifying ESFAS slave relays (assuring 
    equipment operability) will not create any new accident initiators 
    or scenarios. Implementation of the proposed amendment does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        This change does not affect the total ESFAS system response 
    assumed in the safety analysis. The periodic slave relay functional 
    verification is relaxed because of the demonstrated high reliability 
    of the relay and its insensitivity to any short term wear or aging 
    effects. Implementation of the proposed amendment does not result in 
    a reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
    
    [[Page 15999]]
    
        NRC Project Director: Frederick J. Hebdon
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: March 12, 1996
        Brief description of amendments: The proposed amendments would 
    revise Technical Specification (TS) 3/4.6.1.1, ``Containment 
    Integrity,'' 3/4.6.1.2, ``Containment Leakage,'' 3/4.6.1.3, 
    ``Containment Air Locks,'' and 3/4.6.1.6, ``Containment Structural 
    Integrity,'' and add new TS 6.8.3g, ``Containment Leakage Rate Testing 
    Program,'' to implement the new performance-based leakage rate testing 
    program as permitted by 10 CFR Part 50, Appendix J.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes to the TS and the addition of specification 
    6.8.3g to implement the new performance based Containment Leakage 
    Rate Testing Program, have no effect on plant operation. The 
    proposed changes only provide mechanisms within the TS for 
    implementing a performance based methodology for determining the 
    frequency of leak rate testing which has been approved by the 
    Commission. The test type and test method used for testing would not 
    be changed. The test acceptance criteria would not be changed and 
    containment leakage will continue to be maintained within the 
    required limits.
        Directly referencing the Containment Leakage Rate Testing 
    Program for containment [integrated leak rate test] ILRT and [local 
    leak rate test] LLRT requirements does not involve any modification 
    to plant equipment or affect the operation or design basis of the 
    containment. Leakage rate testing is not a precursor to or an 
    initiating event for any accident.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any previously evaluated?
        The proposed changes only allow for the implementation of Option 
    B testing frequencies and do not involve any modifications to any 
    plant equipment or affect the operation or design basis of the 
    containment. The proposed changes do not affect the response of the 
    containment during a design basis accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        The proposed changes do not adversely affect a Safety Limit, 
    Limiting Condition for Operation (LCO) or plant operations. These 
    changes only implement the allowed Option B testing frequencies that 
    have been determined by the Commission not to involve a safety 
    concern. The testing method, acceptance criteria and bases are not 
    changed and still provide assurance that the containment will 
    provide its intended function.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: March 21, 1996
        Description of amendment request: The proposed changes clarify the 
    requirements for testing the charcoal adsorbent in the auxiliary 
    ventilation and control room air filtration systems as outlined in 
    Technical Specifications 4.12 and 4.20, respectively.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
    
        The charcoal testing clarifications and explict reference to the 
    testing currently conducted do not affect system operation or 
    performance, nor do they affect the probability of any event 
    initiators. The changes do not affect any Engineered Safety Features 
    actuation setpoints or accident mitigation capabilities. Therefore, 
    the proposed changes do not significantly increase the consequences 
    of an accident or malfunction of equipment important to safety 
    previously evaluated in the UFSAR [Updated Final Safety Analysis 
    Report].
    
        2. The possibility of an accident or a malfunction of a different 
    type than any previously evaluated is not created.
    
        The clarification to the charcoal sample testing protocol does 
    not affect the method of operation of the system. The proposed 
    changes clarify and explicitly identify the testing methodology for 
    the charcoal samples. No new or different accident scenarios, 
    transient precursors, failure mechanisms, or limiting single 
    failures are introduced as a result of these changes. Therefore, the 
    possibility of a new or different kind of accident other than those 
    already evaluated is not created by this change.
    
        3. The margin of safety has not been significantly reduced.
        The charcoal adsorber sample laboratory testing accurately 
    demonstrates the required performance of the adsorbers following a 
    design basis LOCA [loss-of-coolant accident] or Fuel Handling Accident. 
    Changing the Technical Specifications to clarify the actual test 
    methodology and explicitly [referencing] the charcoal testing actually 
    performed does not affect system performance or operation. Therefore, 
    these changes do not result in a significant reduction in any margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Eugene V. Imbro
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: February 19, 1996
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specifications 
    (TS) Section 4.2 and its associated basis by allowing the application 
    of a voltage-based repair limit for the steam generator tube support 
    plate intersections experiencing
    
    [[Page 16000]]
    outside diameter stress corrosion cracking. The proposed repair 
    criteria are based on guidance provided in Generic Letter 95-05, 
    ``Voltage-Based Repair Criteria for Westinghouse Steam Generator Tubes 
    affected by Outside Diameter Stress Corrosion Cracking,'' dated August 
    14, 1995, and on associated industry guidance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed change was reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed change will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Testing of model boiler specimens for free span tubing (no TSP 
    [tube support plate] restraint) at room temperature conditions show 
    burst pressures in excess of 5,000 psig for indications of ODSCC 
    [outside diameter stress corrosion cracking] with voltage 
    measurements as high as 19 volts. Burst testing performed on five 
    intersections pulled from the Kewaunee SGs [steam generators] with 
    up to a 2 volt indication showed measured tube burst in the range of 
    9,537 to 9,756 psig. Burst testing performed on pulled tubes from 
    other plants with up to 7.5 volt indications show burst pressures in 
    excess of 6,300 psi at room temperatures. Correcting for the effects 
    of temperature on material properties and the minimum strength 
    levels, tube burst capability significantly exceeds the safety 
    factor requirements of RG [Regulatory Guide] 1.121.
        Tube burst criteria are inherently satisfied during normal 
    operating conditions due to the presence of the TSP. Test data 
    indicates that tube burst cannot occur within the TSP, even for 
    tubes with through wall EDM [electro-discharge machining] notches 
    0.75 inch long, when the notch is adjacent to the TSP. Since tube 
    burst is precluded during normal operating conditions, the criterion 
    that must be satisfied to demonstrate adequate tube integrity is a 
    safety margin of 1.43 times MSLB [main steam line break] pressure 
    differential. The BOC [beginning of cycle] structural limit for 7/8 
    inch diameter tubing is 8.82 volts. Applying an allowance of 20.5% 
    for NDE [nondestructive examination] uncertainty and 50% for crack 
    growth rate over an operating cycle results in a voltage repair 
    limit of 5.4 volts. The proposed repair limit of 2 volts is very 
    conservative when compared to the 5.4 volts taking into account the 
    low average growth rates experienced at Kewaunee and the high tube 
    burst pressures.
        Relative to the expected leakage during accident condition 
    loadings, a plant specific calculation was performed to determine 
    the maximum primary-to-secondary leakage during a postulated MSLB 
    event. The evaluation considered both pre-accident and accident 
    initiated iodine spikes. The results of the evaluation show that the 
    accident spike yielded the limiting leak rate. This case was based 
    on a 30 rem thyroid dose at the site boundary and initial primary 
    and secondary coolant activity levels of 1.0 uCi/gm and 0.1 uCi/gm 
    dose equivalent iodine-131, respectively. A leak rate of 34.0 gpm 
    was determined to be the upper limit for allowable primary to 
    secondary leakage in the SG in the faulted loop. The SG in the 
    intact loop was assumed to leak at a rate of 0.1 gpm (150 gpd).
        Application of the voltage-based repair limit will be 
    supplemented with a projected EOC [end of cycle] MSLB leakage 
    calculation and conditional burst probability assessment. The 
    methodology for performing these calculations will be in accordance 
    with the GL [generic letter]. Should the projected MSLB leakage be 
    exceeded indications will be repaired or removed from service until 
    the projected leakage is less than or equal to 34.0 gpm.
        Application of the voltage-based repair limit will not adversely 
    affect SG tube integrity. Therefore, the proposed amendment will not 
    increase the probability or consequences of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Implementation of the proposed voltage-based repair limit will 
    not reduce the overall safety or functional requirements of the SG 
    tube bundles. The tube burst criteria will be satisfied during 
    normal operating conditions by the presence of the TSPs. The RG 
    1.121 criteria that must be satisfied during accident loading 
    conditions is 1.43 times MSLB differential pressure. Conservatively, 
    the existing data base of burst testing shows that the tube burst 
    margins can be satisfied with bobbin coil signal amplitudes of about 
    8.82 volts or less regardless of the depth of tube wall penetration.
        The proposed repair criteria will be supplemented with a reduced 
    operating leakage requirement of 150 gpd through either SG to 
    preclude the potential for excessive leakage during operating 
    conditions. The 150 gpd restriction will provide for timely leakage 
    detection and plant shutdown in the event of the occurrence of an 
    unexpected single crack resulting in leakage that is associated with 
    the longest permissible crack length. The operating leakage limit is 
    based on leak-before break considerations, critical crack length and 
    predicted leakage.
        The SG tube integrity will continue to be maintained through 
    inservice inspections and primary-to-secondary leakage monitoring. 
    Therefore, the proposed change will not create the possibility of a 
    new or different kind or accident.
        3. Involve a significant reduction in the margin of safety.
        Application of the voltage-based repair criteria has been 
    demonstrated to maintain tube integrity commensurate with the RG 
    1.121 criteria. RG 1.121 describes a method acceptable to the staff 
    for meeting GDCs [general design criteria] 2, 14, 15, 31 and 32. 
    This is accomplished by determining the limiting degradation of SG 
    tubing as established by inservice inspection, beyond which tubes 
    should be removed from service. Upon implementation of the repair 
    criteria, even under the worst case conditions, the occurrence of 
    ODSCC at the TSPs is not expected to lead to a SG tube rupture event 
    during normal or faulted conditions. The most limiting event would 
    be a potential increase in leakage during a MSLB event. Excessive 
    leakage during a MSLB is precluded by verifying that the expected 
    EOC crack distribution of ODSCC indications at TSP locations would 
    result in an acceptably low primary-to-secondary leakage. Therefore, 
    the radiological consequences from tubes remaining in service is a 
    small fraction of the 10 CFR 100 limits.
        The combined effects of a LOCA [loss-of-coolant accident] plus 
    SSE [safe shutdown earthquake] on the SGs were assessed as required 
    by GDC 2. This issue was addressed for the Kewaunee SGs through the 
    application of leak-before-break (LBB) principles to the primary 
    loop piping. Based on the results of this analysis, it is concluded 
    that the LBB is applicable to the Kewaunee primary loops and, thus, 
    the probability of breaks in the primary loop piping is sufficiently 
    low that they need not be considered in the structural design basis 
    of the plant. Excluding breaks in the primary loops, the LOCA loads 
    from the large branch lines were also assessed and found to be of 
    insufficient magnitude to result in SG tube collapse. Based on these 
    analysis results, no tubes are expected to collapse or deform to the 
    degree that the secondary-to-primary in-leakage would be increased 
    over currently expected levels. On this basis no tubes need to be 
    excluded from the voltage-based repair criteria for reasons of 
    deformation resulting from combined LOCA or SSE loadings.
        Addressing the RG 1.83 considerations, implementation of the 
    voltage-based repair criteria will include a 100% bobbin coil probe 
    inspection of all tube-to-TSP intersections with known ODSCC down to 
    the lowest cold leg TSP identified. This will be supplemented by a 
    reduced operating leakage limit, enhanced eddy current data analysis 
    guidelines, MRPC [motorized rotating pancake coil] inspection 
    requirements and a projected EOC voltage distribution. It is 
    concluded that the proposed change will not result in a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497
        NRC Project Director: Gail H. Marcus
        
    [[Page 16001]]
    
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: January 16, 1996
        Brief description of amendments: The amendments revise the 
    Technical Specifications to reflect approval of the use of 10 CFR Part 
    50, Appendix J, Option B, for the Calvert Cliffs Nuclear Power Plant, 
    Unit Nos. 1 and 2, containment leakage rate test program for Type A 
    tests only.
        Date of issuance: March 13, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 212 and 189
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5810) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated March 13, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2 Calvert 
    County, Maryland
    
        Date of application for amendments: November 30, 1995, as 
    supplemented by letter dated March 15, 1996.
        Brief description of amendments: The amendments allow the 
    installation of tube sleeves as an alternative to plugging for repair 
    of steam generator (SG) tubes using repair techniques developed by 
    Westinghouse Electric Corporation. The November 30, 1995, letter also 
    requested approval of repair techniques developed by ABB Combustion 
    Engineering, Inc., for repairing SG tubes. The NRC staff is still 
    reviewing that portion of the request and will notice the results of 
    its review at a future date.
        Date of issuance: March 22, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 213 and 190
        Facility Operating License No. DPR-53 and DPR-69: Amendment revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    176) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated March 22, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: November 22, 1995
        Brief description of amendment: The proposed change will delete the 
    qualifying statement, ''... provided the remaining systems are in 
    continuous operation,'' from TS Section 3.3.4.2.
        Date of issuance: March 15, 1996
        Effective date: March 15, 1996
        Amendment No. 168
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 6, l995 (60 FR 
    62487) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 15, 1996No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: July 18, 1994, as supplemented 
    by letters dated October 9, 1995, February 13 and March 8, 1996
        Brief description of amendments: The amendments revise the current 
    combined Technical Specifications (TS) for Units 1 and 2 by separating 
    them into individual volumes for Unit 1 and Unit 2. In addition to the 
    changes required by the TS split, some administrative and editorial 
    changes were made, such as the correction of typographical errors and 
    the deletion of unnecessary blank pages.
        Date of issuance: March 21, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: Unit 1 - 166 - Unit 2 - 148
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 14, 1994 (59 
    FR 47166) The October 9, 1995, February 13 and March 8, 1996, letters 
    provided additional information that did not change the scope of the 
    July 18, 1994, application and the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    March 21, 1996 and Environmental Assessment dated February 7, 1996. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    [[Page 16002]]
    
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: December 15, 1995, as 
    supplemented March 5, 1996
        Brief description of amendments: These amendments (1) revise 
    Technical Specifications (TSs) 3/4.6.1.1, 3/4.6.1.2, 3/4.6.1.3, 3/
    4.6.1.6, and associated Bases, (2) delete TS 6.9.2.g, and (3) add a new 
    TS 6.17. These changes make the TSs consistent with Option B of 
    Appendix J of 10 CFR Part 50 and the implementing guidance of 
    Regulatory Guide 1.163, ``Performance-Based Containment Leak Test 
    Program,'' dated September 1995. Option B of Appendix J permits 
    implementation of a performance-based leak rate test schedule in lieu 
    of the prescriptive requirements contained in Option A of Appendix J. 
    These amendments remove from the TSs the prescriptive requirements of 
    Option A concerning test frequencies and test methodology. These 
    amendments also include minor administrative and editorial changes to 
    add consistency between the Bases and the TSs and provide additional 
    clarification.
        Date of issuance: March 19, 1996
        Effective date: Both units, as of the date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 197 and 80
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    179) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 19, 1996.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. 
    Lucie Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of application for amendment: August 16, 1995
        Brief description of amendment: This amendment modifies Technical 
    Specification 3.6.6.1, Shield Building Ventilation System (SBVS), to 
    more effectively address the design functions performed by the SBVS for 
    both the Shield Building and the Fuel Handling Building.
        Date of issuance: March 20, 1996
        Effective date: March 20, 1996
        Amendment No.: 81
        Facility Operating License No. NPF-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49937) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 20, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mill 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: August 10, 1995, as supplemented 
    on December 21, 1995, and February 22, 1996
        Brief description of amendment: The amendment deletes a Technical 
    Specification (TS) reference to the reactor trip input to the reactor 
    building isolation system, changes the surveillance frequency for the 
    sodium hydroxide storage tank and station battery, and removes an 
    inappropriate reference in the TS bases section to testing that is not 
    required by the TSs themselves.
        Date of issuance: March 21, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 200
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 27, 1995 (60 
    FR 58401). The December 21, 1995 and February 22, 1996 letters did not 
    change the staff's determination hazards consideration exist. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated March 21, 1996No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: December 19, 1995 and 
    supplemented February 16, 1996 (AEP:NRC:1215B&D)
        Brief description of amendments: The amendments modify the 
    technical specifications to replace the existing scheduling 
    requirements for overall integrated and local containment leakage rate 
    testing with a requirement to perform the testing in accordance with 10 
    CFR Part 50, Appendix J, Option B. Option B allows test scheduling to 
    be adjusted based on past performance.
        Date of issuance: March 19, 1996
        Effective date: March 19, 1996, with full implementation within 45 
    days
        Amendment Nos.: Unit 1 - 209, Unit 2 -193
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1632) The February 16, 1996 supplement made only a minor change to the 
    proposed technical specifications that provided consistency between the 
    wording for Units 1 and 2. The change did not affect the staff's 
    proposed finding that the amendments involve no significant hazards 
    consideration.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 19, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Maud Preston Palenske 
    Memorial Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: February 17, 1996
        Brief description of amendment: The amendment allows one main steam 
    line's leakage rate to be as high as 35 standard cubic feet per hour 
    (scfh) as long as the total leakage through all four main steam lines 
    does not exceed 100 scfh until the end of Operating Cycle 6.
        Date of issuance: March 18, 1996
        Effective date: March 18, 1996
        Amendment No.: 83
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications. The Commission's related evaluation of the 
    amendment and final no significant hazards consideration determination 
    is contained in a Safety Evaluation dated March 18, 1996. Public 
    comments requested as to proposed no significant hazards consideration: 
    Yes (61 FR 7823 dated February 29, 1996). That notice provided an 
    opportunity to submit comments on the Commission's
    
    [[Page 16003]]
    proposed no significant hazards consideration determination. No 
    comments have been received. The notice also provided for an 
    opportunity to request a hearing by April 1, 1996, but indicated that 
    if the Commission makes a final no significant hazards consideration 
    determination any such hearing would take place after issuance of the 
    amendment.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: December 19, 1994 (TXX-94274), as 
    supplemented by letter dated January 25, 1996 (TXX-96026)
        Brief description of amendments: These changes allowed testing of 
    Reactor Protection System and Engineered Safety Features Actuation 
    System instrument channels with the channel under test in bypass in 
    order to reduce the vulnerability to spurious trips during surveillance 
    testing.
        Date of issuance: March 14, 1996
        Effective date: March 14, 1996
        Amendment Nos.: Unit 1 - 47; Unit 2 - 33
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6312) The additional information contained in the supplemental letter 
    dated January 25, 1996, was clarifying in nature and thus, within the 
    scope of the initial notice and did not affect the staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated March 14, 1996. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment requests: November 21, 1995 (TXX-95289), as 
    supplemented by letters dated February 22 (TXX-96061 and TXX-96062) and 
    28, (TXX-96068), and March 13, 1996 (TXX-96090).
        Brief description of amendments: The amendments allowed both doors 
    of the containment personnel airlock to be open during fuel movement 
    and core alterations, providing one airlock door is capable of being 
    closed and the water level in the refueling pool is maintained.
        Date of issuance: March 18, 1996
        Effective date: March 18, 1996
        Amendment Nos.: Unit 1 - 48; Unit 2 - 34
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    185) The additional information contained in the supplemental letters 
    dated February 22 (2 letters) and 28, and March 13, 1996, were 
    clarifying in nature and thus, within the scope of the initial notice 
    and did not affect the staff's proposed no significant hazards 
    consideration determination.The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated March 18, 1996.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: May 26, 1994, as supplemented 
    January 5, April 25 and October 12, 1995, and February 2 and March 1, 
    1996.
        Brief description of amendments: These amendments revise the 
    Technical Specifications by extending the operation of both units with 
    the current heatup and cooldown limit curves to 23.6 effective full 
    power years. The basis for TS Section 15.3.1.B, ``Pressure/Temperature 
    Limits,'' is also revised to reflect the methodology for the curve 
    compilation.
        Date of issuance: March 20, 1996
        Effective date: March 20, 1995
        Amendment Nos.: 168 and 172
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37093). The supplemental submittals provided additional information 
    that did not change the initial proposed no significant hazards 
    consideration determination.The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated March 20, 1996.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been
    
    [[Page 16004]]
    issued without opportunity for comment. If there has been some time for 
    public comment but less than 30 days, the Commission may provide an 
    opportunity for public comment. If comments have been requested, it is 
    so stated. In either event, the State has been consulted by telephone 
    whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By May 10, 1996, the licensee 
    may file a request for a hearing with respect to issuance of the 
    amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be
    
    [[Page 16005]]
    granted based upon a balancing of the factors specified in 10 CFR 
    2.714(a)(1)(i)-(v) and 2.714(d).
    
    Arizona Public Service Company, et al., Docket No. STN 50-529, Palo 
    Verde Nuclear Generating Station, Unit 2, Maricopa County, Arizona
    
        Date of application for amendment: March 23, 1996
        Brief description of amendment: The amendment modifies Technical 
    Specification (TS) 4.8.2.1.c, ``DC Sources - Operating,'' to specify 
    that the provisions of TS 4.0.1 and 4.0.4 are not applicable. This 
    provision expires upon entry into Mode 4 coming out of the sixth 
    refueling outage or upon any deep discharge cycle of the battery.
        Date of issuance: March 23, 1996
        Effective date: March 23, 1996
        Amendment No.: Unit 2 - 94
        Facility Operating License No. NPF-51: The amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No.The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 23, 1996.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq. Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
    
    Arizona Public Service Company, et al., Docket No. STN 50-529, Palo 
    Verde Nuclear Generating Station, Unit 2, Maricopa County, Arizona
    
        Date of application for amendment: March 26, 1996
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3/4.9.6 to allow the refueling machine overload 
    cutoff limit to be increased to as much as 2000 pounds, from the 
    current 1600 pound limit, in an effort to free the stuck fuel assembly 
    from core location A-06. The additional 400 pound increase will be 
    applied in 50 pound increments. This change will expire when the fuel 
    assembly located at core location A-06 is successfully withdrawn.
        Date of issuance: March 26, 1996
        Effective date: March 26, 1996, to be implemented prior to entry 
    into Mode 4 from the current refueling outage.
        Amendment No.: Unit 2 - 95
        Facility Operating License No. NPF-51: The amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No.The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 26, 1996.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq. Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: March 29, 1996
        Brief description of amendment: The amendment clarifies the testing 
    requirements and updates the regulatory and industry guidance 
    references for charcoal adsorber units addressed by TS 4.6.4.4, 
    Hydrogen Purge System; TS 4.6.5.1, Emergency Ventilation System; and TS 
    4.7.6.1, Control Room Emergency Ventilation System.
        Date of issuance: March 29, 1996
        Effective date: March 29, 1996
        Amendment No.: 209
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No.The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 29, 1996.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
        Dated at Rockville, Maryland, this 3rd day of April 1996.
    
        For the Nuclear Regulatory Commission.
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 96-8786 Filed 4-9-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
04/10/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-8786
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
15985-16005 (21 pages)
PDF File:
96-8786.pdf