95-8845. Biweekly Notice  

  • [Federal Register Volume 60, Number 70 (Wednesday, April 12, 1995)]
    [Notices]
    [Pages 18621-18640]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-8845]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 17, 1995, through March 31, 1995. The 
    last biweekly notice was published on March 29, 1995 (60 FR 16181).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve [[Page 18622]] no significant hazards 
    consideration. Under the Commission's regulations in 10 CFR 50.92, this 
    means that operation of the facility in accordance with the proposed 
    amendment would not (1) involve a significant increase in the 
    probability or consequences of an accident previously evaluated; or (2) 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated; or (3) involve a significant reduction 
    in a margin of safety. The basis for this proposed determination for 
    each amendment request is shown below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By May 12, 1995, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram [[Page 18623]] Identification Number N1023 and 
    the following message addressed to (Project Director): petitioner's 
    name and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IllinoisDocket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: March 23, 1994, as supplemented on July 
    26, 1994, February 15, 1995, and February 28, 1995.
        Description of amendment request: In the submittals of March 23 and 
    July 26, 1994, the licensee requested revisions to the plants' 
    technical specifications (TSs) to permit the use of a slightly positive 
    reactor core moderator temperature coefficient (MTC). The February 15, 
    1995, submittal requested approval to expand the operating limits 
    report (OLR) to include a cycle specific MTC value and requested 
    approval to maintain the MTC value within the limits specified in the 
    OLR. The maximum upper MTC limit would be specified in the TSs. The 
    February 28, 1995, submittal provided a revised Significant Hazards 
    Consideration. This supplements the information that was published in 
    the Federal Register on August 31, 1994 (59 FR 45037).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        An analysis program was pursued by Commonwealth Edison to 
    justify a positive MTC, reduced reactor coolant system thermal 
    design flow, and increased steam generator tube plugging levels. 
    This analysis identified a need for corresponding increases in the 
    boron concentration levels in the refueling water storage tank 
    (RWST) and safety injection accumulators to assure subcriticality 
    requirements are met following a postulated loss-of-coolant accident 
    (LOCA). The increases in boron concentration are based on the 
    maximum upper limit of the MTC. The corresponding Technical 
    Specification changes required as a result of this analysis program 
    were previously approved by the NRC, including the increases in 
    boron concentration limits, with the exception of the positive MTC 
    change. The safety analyses necessary to support this program are 
    documented in WCAP-13964. The results were reviewed by Commonwealth 
    Edison and found to be acceptable. All Departure from Nucleate 
    Boiling Ratio (DNBR) design limits were determined such that there 
    was a 95 percent probability at a 95 percent confidence level that 
    DNB would not occur on the most limiting fuel rod for any Condition 
    I or Condition II event. The present Technical Specification limit 
    for Nuclear Enthalpy Rise Hot Channel Factor, ... , of less than 
    1.65 ensures that the DNB design basis stated above would be met, 
    thus fuel integrity will not be challenged.
        The accidents which are sensitive to MTC were analyzed as part 
    of the overall program and the results were found to be acceptable. 
    The safety functions of the evaluated systems and components remain 
    unchanged. The analysis performed using the increased MTC value does 
    not affect the integrity of the safety related systems and 
    components such that their function to control radiological 
    consequences is affected and all fission barriers will remain 
    intact. The effects on offsite doses have been considered. The 
    incorporation of a positive MTC, in conjunction with the previously 
    approved reduction in reactor coolant system thermal design flow 
    rate and increase in steam generator tube plugging levels, will 
    result in a small increase in offsite doses; however, the total 
    doses remain a small fraction of the 10 CFR 100 limits. As such, the 
    accident analysis acceptance criteria continue to be satisfied.
        On a cycle-by-cycle basis, a deterministic evaluation of the 
    impact on ATWS risk will be performed. An Unfavorable Exposure Time 
    (UET) will be calculated, where UET is defined as the amount of time 
    during the operating cycle for which the reactivity feedback is not 
    sufficient to prevent Reactor Coolant System (RCS) pressure from 
    exceeding 3200 psig for a given plant configuration. The UET 
    methodology is consistent with the Westinghouse Owner's Group 
    methodology presented in WCAP 11992, ``ATWS Rule Administration 
    Process'' and WCAP 11993, ``Assessment of Compliance with ATWS Rule 
    Basis for Westinghouse PWRs''. Corrective actions will be taken, as 
    necessary, to assure a UET of less than 5 percent of cycle length.
        The relocation of the cycle-specific core operating limits for 
    the MTC from the Technical Specifications has no influence or impact 
    on the probability or consequences of any accident previously 
    evaluated. Byron and Braidwood Stations will continue to operate 
    within the cycle-specific MTC limits contained in the OLR. The 
    proposed amendment will require exactly the same action to be taken 
    when the OLR limits are exceeded as are required by the current 
    Technical Specification. Any change to the MTC values in the OLR 
    will be performed based on NRC-approved methodology as delineated in 
    Section 6.9.1.9 of the Technical Specifications. Each accident 
    analysis addressed in the Updated Final Safety Analysis Report 
    (UFSAR) will be examined with respect to changes in cycle dependent 
    parameters, which are obtained from application of NRC-approved 
    reload design methodologies, to ensure that the transient evaluation 
    of new reloads are bounded by previously accepted analysis. This 
    examination, which will be performed under the requirements of 10 
    CFR 50.59, ensures that future reloads will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        Therefore, implementation of a positive MTC will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different type of accident from any accident previously 
    evaluated.
        The methodology and manner of plant operation as a result of the 
    proposed changes is unaffected. Implementation of a positive MTC 
    does not impact the safe operation of the reactor provided that the 
    Limiting Conditions for Operation (LCOs) and the associated action 
    requirements are satisfied. The assumptions do not create any new 
    failure modes that could adversely impact safety related equipment. 
    The reload safety limits and LCOs in the plant Technical 
    Specifications will be evaluated and satisfied for each future 
    reload core design via the 10 CFR 50.59 process. All DNBR limits 
    have been satisfied. Currently installed equipment will not be 
    operated in a manner different than previously designed. No new 
    credible limiting single failure has been created. No new or 
    different accidents or failure modes have been identified for any 
    systems or components important to safety.
        The relocation of the cycle specific MTC values to the OLR will 
    not create the possibility of a new or different type of accident. 
    No safety related equipment or safety function will be altered as a 
    result of this proposed change. The cycle specific values are 
    calculated using NRC-approved methods and submitted to the NRC to 
    allow the Staff to continue to trend these limits. The Technical 
    Specifications will continue to require operation within the 
    analyzed core operating limits and appropriate actions will be 
    taken, when, or if, the limits are exceeded. [[Page 18624]] 
        Therefore, there is not a potential for creating the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The performance and integrity of the evaluated safety related 
    systems and components are not affected by the proposed change to 
    the MTC. The radiological consequences of all previously analyzed 
    accidents remain within acceptable limits. The proposed change to 
    the MTC will have no effect on the availability, operability, or 
    performance of the evaluated safety related systems or components. 
    The incorporation of a positive MTC, in conjunction with the 
    previously approved reduction in reactor coolant system thermal 
    design flow rate and increase in steam generator tube plugging 
    levels, will result in a small increase in offsite doses; however, 
    the total doses remain a small fraction of the 10CFR100 limits. The 
    methodology, discussed in Attachment E, describes the determination 
    and use of the UET values in the calculation of the Primary Pressure 
    Relief node for the ATWS event tree to determine an overall ATWS 
    risk value. The methodology will be used by ComEd to ensure that a 
    core designed with a positive MTC will not result in an unacceptable 
    risk to core damage frequency due to an ATWS event. The margin of 
    safety associated with the licensing basis safety analysis is not 
    significantly reduced by the proposed changes. All acceptance 
    criteria for the specific UFSAR Chapter 15 safety analyses (non-LOCA 
    and LOCA) have been satisfactorily evaluated and verified using NRC 
    approved methodologies.
        The margin of safety is not affected by the relocation of the 
    cycle specific MTC limits from the Technical Specifications. The 
    proposed amendment continues to require operation within the core 
    limits as determined by the NRC-approved reload design and safety 
    analysis methodologies. Appropriate actions will be taken, when, or 
    if, limits are exceeded.
        The development of the MTC limits for future reloads will 
    continue to conform to those methods described in the NRC-approved 
    documentation. In addition, each future reload will involve a 10 CFR 
    50.59 safety review to assure that operation of the unit within the 
    cycle specific limits will not involve a reduction in the margin of 
    safety as defined in the basis for any Technical Specification.
        Therefore, there is no significant reduction in the margin of 
    safety as defined in the bases of any Technical Specification.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: Robert A. Capra
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of amendment request: October 20, 1992
        Description of amendment request: The proposed amendment would 
    comply with the requirements of Amendment 135 to the Palisades 
    Operating License, dated February 11, 1991, which included a change to 
    Technical Specification 5.3.1a, Primary Coolant System. The safety 
    evaluation for Amendment 135 included a requirement that changes to 
    Section 4.2 of the Palisades Final Safety Analysis Report (FSAR) be 
    made through a formal amendment process. The proposed FSAR change is a 
    result of the steam generator replacement project and includes the 
    following: (1) deletion of a design load since this was not treated as 
    a necessary design condition in the new steam generators; (2) a change 
    in the feedwater temperature from 70 deg.F to 40 deg.F, since this 
    assumption was changed in the analysis for the replacement steam 
    generators; and (3) editorial changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The following summary supports the finding that the proposed 
    change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The probability of an accident previously evaluated in the FSAR 
    will not be increased by deleting the design load change of 15% per 
    minute or decreasing the minimum feedwater temperature from 70 deg.F 
    to 40 deg.F. There is no design requirement that the plant be 
    capable of 15% per minute load changes. No accident has as an 
    initial condition a 15% per minute load change taking place, and 
    since this FSAR change is the result of the replacement steam 
    generators design, no accident probabilities are increased. The 
    40 deg.F feedwater temperature affects the steam generators, but 
    nothing else is affected in the primary coolant system (PCS). The 
    replacement steam generators have been shown by the design analysis 
    report to be able to withstand the same number of cycles of the 
    addition of 40 deg.F water as the old steam generators could with 
    70 deg.F water.
        The consequences of an accident previously evaluated in the FSAR 
    are not increased by either of these two changes. Deleting the 
    design load rate of 15% per minute deals with normal plant operation 
    and would not affect the course of a Chapter 14 event since none of 
    the Chapter 14 events involve power level changes with respect to 
    the steam generators. Also, reducing the maximum design load change 
    rate is a conservative change.
        Lowering the feedwater temperature could increase the 
    consequences of the main steam line break (MSLB) accident by 
    increasing the likelihood of a return to power event caused by 
    increased core cooling; however, the current FSAR analysis in 
    Section 14.14 used 32 deg.F as the auxiliary feedwater temperature 
    and thus bounds [the] 40 deg.F [temperature].
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The possibility of a new or different type of accident is not 
    created by these FSAR changes. By deleting the 15% per minute load 
    change rate from the FSAR, the operation of the plant is unaffected 
    because the 5% per minute limit on load rate change is more 
    limiting. There is no license requirement to be able to change power 
    at 15% per minute except as described in the proposed FSAR deletion. 
    Furthermore, FSAR Section 4.3.7.2 states that the pressurizer 
    heaters cannot be uncovered by the outward surge of water following 
    load increases; a 10% step increase and 15% ramp increase. FSAR 
    Section 1.2.4.9.a states that the nuclear steam supply system (NSSS) 
    is capable of a ramp change from 15% to 100% power at 5% per minute, 
    and at a greater rate over smaller load changes up to a step change 
    of 10%.
        Another consideration is that the analysis for the original 
    steam generators was not as detailed or exact as the analysis for 
    the replacement steam generators. The thermal analysis section of 
    the original steam generator design analysis report states for the 
    three power change cases, 5% per minute, 15% per minute and a 10% 
    step change, that ''... the transient thermal effects of the power 
    changes are small and [negligible]. The situations of significance 
    are due to cycling between steady state conditions at different 
    power levels.'' Thus, the rate of change was not a consideration in 
    the original design analysis. The replacement steam generator 
    analysis calculated the transient temperature changes with respect 
    to time, so the rate of change was considered. Therefore, the 
    replacement steam generator analysis is more accurate, but does not 
    consider a 15% per minute rate change. The original steam generators 
    were not designed for 15% per minute power changes but could 
    withstand power increases from 50% to 100% [a total of] 15,000 times 
    without considering the rate of power change.
        Reducing the analyzed feedwater temperature from 70 deg.F to 
    40 deg.F does not change the possibility of whether another type of 
    accident or malfunction can occur since the steam generator is 
    analyzed for this.
        3. Involve a significant reduction in a margin of safety.
        The margin of safety as defined by plant licensing basis is not 
    reduced due to the replacement steam generators not being analyzed 
    for a 15% per minute power ramp [[Page 18625]] because the 15% per 
    minute ramp rate was not a licensing basis of the plant design. The 
    original plant Safety Evaluation Report does not mention the design 
    power ramp rates. The basis for Technical Specification 3.1.2 states 
    that all components are designed to withstand the effects of cyclic 
    loads due to primary coolant system temperature and pressure changes 
    induced by load changes, trips, and start-ups and shutdowns. FSAR 
    Section 4.2.2 is referenced. The change of eliminating the analyzed 
    ability to make 15% per minute power changes does not reduce the 
    margin of safety because:
        a. the plant is not operated in a manner wherein 15% per minute 
    power increases are made. Rapid power decreases during emergency 
    conditions are not covered by this analysis since they are not 
    controlled to 15% per minute but should be considered analyzed by 
    the 500 trips or 10% step change analysis and,
        b. the original steam generator did not use the ramp rate in the 
    analysis and,
        c. a 15% per minute power change from 50% to 100% power is a 
    fairly benign change for the steam generator with respect to 
    pressure and temperature changes as compared to heatups and 
    cooldowns because the total changes are small.
        The only requirement from the NRC with respect to the number and 
    type of loads is contained in Section II of the NRC Standard Review 
    Plan (SRP) 3.9.1 which states ''...The section of the applicant's 
    SAR which pertains to transients will be acceptable if the transient 
    conditions selected for equipment fatigue evaluation are based upon 
    a conservative estimate of the magnitude and frequency of the 
    temperature and pressure conditions resulting from those 
    transients.'' ''... Transients and resulting loads and load 
    combinations with appropriate specified design and service limits 
    must provide a complete basis for design of the reactor coolant 
    pressure boundary for all conditions and events expected over the 
    service lifetime of the plant.''
        In the intervening years between design of the original steam 
    generators and the replacement steam generators, Combustion 
    Engineering (ABB-CE) decided that a 15% per minute power ramp rate 
    was beyond what was necessary and expected to occur. This position 
    was acceptable to the NRC since ABB-CE letter CPC-90-170, dated 
    October 24, 1990, states that the replacement steam generators are 
    identical in design to the Palo Verde (Arizona Public Service) steam 
    generators. (The ABB-CE letter was concerned with the stress 
    analysis for steam line breaks, therefore, the reference to being 
    identical was with respect to that stress analysis.)
        The change in feedwater temperature from 70 deg.F to 40 deg.F 
    maintains the margin of safety because the replacement steam 
    generators have been shown by the design analysis report to be able 
    to withstand the same number of cycles of the addition of 40 deg.F 
    water as the old steam generators could 70 deg.F water.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201
        NRC Project Director: Cynthia A. Carpenter, Acting
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: September 13, 1993
        Description of amendment request: The proposed amendment would 
    relocate audit frequencies of Section 6.5.2.8 of the Technical 
    Specifications to the Quality Assurance Program in Section 17.2 of the 
    Updated Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change to relocate the audit program frequency 
    requirements to the Quality Assurance Program does not:
        (1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated,
        This change is administrative in nature and does not impact the 
    operation of the plant or the plant's response to an accident. 
    Because it will allow more flexibility in assigning resources to 
    assess weak or declining performance areas, the plant safety 
    performance will be improved.
        (2) create the possibility of a new or different kind of 
    accident from any accident previously evaluated,
        This change is administrative in nature and does not affect the 
    operation or design of the plant; therefore, there is no change in 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        (3) involve a significant reduction in a margin of safety.
        This change is administrative in nature and does not affect the 
    operation of the plant; therefore, there is no change in the margin 
    of safety. Relocating the audit program frequency requirements to 
    the Quality Assurance program will allow a more dynamic and 
    responsive audit program. Audits will be able to be scheduled more 
    effectively based on performance and the status of related 
    activities. This should result in a more effective audit program 
    that will contribute to an improvement in safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226
        NRC Project Director: Cynthia A. Carpenter, Acting
    
    Entergy Operations, Inc., Docket Nos. 50-313 and 50-368, 
    ArkansasNuclear One, Unit Nos. 1 and 2 (ANO-1&2), Pope County, 
    Arkansas
    
        Date of amendment request: August 30, 1994, with supplement dated 
    January 19, 1995.
        Description of amendment request: The proposed amendment changes 
    requirements related to the site parimeter security system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, excerpts of this analysis are presented below:
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated
        The accident mitigation features of the plant are not affected 
    by the proposed change. This change provides an equivalent level of 
    protection as required by 10CFR73.55(c)(4), does not significantly 
    decrease the effectiveness of the security program, and is adequate 
    for preventing an unacceptable risk to public health and safety. 
    Ample protection against a design basis security threat continues to 
    be provided. Therefore, the probability or consequences of an 
    accident previously evaluated is not significantly increased.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from Any Previously Evaluated
        This change clarifies the existing configuration of the 
    protected area barrier at the ANO intake structure. New systems, 
    modes of equipment operation, failure modes, or other plant 
    perturbations are not introduced by this change. Therefore, the 
    possibility of a new or different kind of accident from amy 
    previously evaluated is not created.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety
        This change clarifies the existing configuration of the 
    protected area barrier at the ANO intake structure. The proposed 
    change does not alter a safety limit, a limiting condition of 
    operation, or a surveillance requirement on equipment to operate the 
    plant. Adequate physical protection of the plant is maintained. 
    Therefore, the margin of safety is not significantly 
    reduced. [[Page 18626]] 
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center 
    (DAEC), Linn County, Iowa
    
        Date of amendment request: March 1, 1995
        Description of amendment request: The proposed License Amendment 
    would revise Technical Specification (TS) Sections 4.5 and 4.8 of the 
    DAEC TS to reflect the changes to pump and valve testing criteria. The 
    proposed amendment changes the testing frequency for certain pumps and 
    valves in the Low Pressure Coolant Injection subsystem; Core Spray 
    subsystems; and the Residual Heat Removal Service Water, High Pressure 
    Coolant Injection, Emergency Service Water, and River Water Supply 
    systems. The frequency would change from testing every three months to 
    that specified by DAEC ASME Section XI Inservice Testing (IST) program.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The affected pumps and valves in Sections 4.5 and 4.8 will 
    continue to be tested in accordance with ASME Section XI OM-6 and 
    OM-10. The affected pumps and valves will continue to function as 
    before and this change will not result in a decrease in their 
    availability to mitigate the consequences of certain accidents and 
    transients. The proposed amendment will not affect the consequences 
    of these accidents and transients. Therefore, the
        proposed amendment does not involve a change in the probability 
    or consequences of an accident previously evaluated.
        (2) The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated. The safety functions of the affected pumps and 
    valves will remain unchanged. This amendment will result in no 
    physical changes to the affected pumps, valves or systems. 
    Consequently, the proposed license amendment does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        (3) The proposed amendment will not reduce the margin of safety. 
    The actual operation of the affected pumps and valves will remain 
    unchanged. Testing in accordance with ASME Section XI OM-6 and OM-10 
    will continue to provide assurance that degradation in tested 
    components will be detected and addressed.
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401
        Attorney for licensee: Jack Newman, Kathleen H. Shea, Morgan, Lewis 
    & Bockius, 1800 M Street, N.W., Washington, DC 20036-5869NRC Acting 
    Project Director: Gail H. Marcus
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: January 24, 1995, as supplemented March 
    22, and March 29, 1995.
        Description of amendment request: The amendment request would 
    revise the Technical Specification Section 3.2.3.1.a and Table 2.2-1 to 
    decrease the acceptance criterion for measured reactor coolant system 
    (RCS) flow rate from 387,480 gallons per minute (gpm) to 371,920 gpm.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
        ...The proposed changes do not involve an SHC because the 
    changes would not:
        1. Involve a Significant Increase in the Probability or 
    Consequence of an Accident Previously Evaluated.
        An evaluation of the 4% decrease in the RCS total flow rate 
    limit has shown that the change does not significantly impact the 
    design basis analyses. Therefore, the change will not increase the 
    consequences of an accident previously evaluated.
        There are no actual plant changes that will result from this 
    technical specification change. Instead, the technical specification 
    requirement for minimum total RCS flow rate is being changed to 
    provide operational benefit without compromising safety. Since there 
    are no plant changes, there is no effect on the probability of 
    occurrence of previously evaluated accidents.
        The change will have a negligible impact on the small break loss 
    of coolant accident (LOCA) and large break LOCA analyses. The PCT 
    [peak cladding temperature] acceptance criteria will continue to be 
    met with the assumption of a 4% reduction in RCS flow rate.
        For the steam generator tube rupture event, both the FSAR [Final 
    Safety Analysis Report] offsite dose analysis and the margin of 
    steam generator (SG) overfill were evaluated. It was determined that 
    the 4% reduction in RCS flow rate will not adversely affect the 
    offsite doses or the margin to SG overfill and, therefore, the FSAR 
    conclusions remain unchanged.
        In the evaluation of non-LOCA transients, the DNB [departure 
    from nucleate boiling] is the most affected parameter due to a 
    change in flow rate. It was concluded that the 4% reduction in RCS 
    flow was acceptable and there was margin to the DNB limit.
        It is concluded that there is sufficient margin to the system 
    pressure, PCT and DNB limits to offset the effect of the 4% flow 
    rate decrease and the calculated radiological releases associated 
    with the analysis are not affected. Therefore, there is no effect on 
    the consequences of previously evaluated accidents.
        2. Create the Possibility of a New or Different Kind of Accident 
    from any Previously Evaluated.
        The low loop flow trip setpoint specified in Technical 
    Specification Table 2.2-1 is set as a fraction of total flow. The 
    flow fraction is not being changed and no hardware changes are 
    required due to the reduction in minimum flow. Also, the reduction 
    in minimum flow will not change the operation of any plant equipment 
    and it does not modify plant operation.
        Therefore, the reduction in minimum flow does not introduce any 
    new failure modes or malfunctions and it does not create the 
    potential for a new unanalyzed accident.
        3. Involve a Significant Reduction in the Margin of Safety.
        The proposed 4% decrease in the technical specification limit 
    for total RCS flow rate will not adversely affect the results of the 
    FSAR accident analysis, and it is concluded that this change is 
    safe. The change does not adversely affect any equipment credited in 
    the safety analysis, and it does not affect the probability of 
    occurrence of any plant accident. Also, the change has a negligible 
    impact on the PCT, and it does not increase the offsite doses or 
    decrease the DNB below its acceptance limit.
        Therefore, the change does not have any significant impact on 
    the protective boundaries, and there is no reduction in the margin 
    of safety as specified in the technical specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 
    [[Page 18627]] New London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station,Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: March 1, 1995
        Description of amendment request: The proposed amendment to the 
    technical specifications (TS) would make administrative changes to TS 
    2.5, 2.8, 2.11, 3.2, and 3.10 and, in accordance with Generic Letter 
    (GL) 93-07, ``Modification of the Technical Specification 
    Administrative Control Requirements for Emergency and Security Plans,'' 
    to TS 5.5 and 5.8.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed revisions to Technical Specifications (TS) 5.5 and 
    5.8 are administrative in nature and follow the guidance of Generic 
    Letter (GL) 93-07. The review and audit functions of the site 
    security and emergency plans and procedures will be retained in a 
    manner that fully satisfies regulatory requirements. Therefore, the 
    proposed revisions do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed revision to TS 2.5 will still require backup water 
    for the emergency feedwater storage tank to be available. However, 
    several other available sources of water are preferred over river 
    water, such as, the water plant demineralized water system and the 
    outside condensate storage tank. Therefore, the proposed revision 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed deletion of TS 2.8(8) pertaining to fuel handling 
    cranes, deletion of TS 2.11 pertaining to overhead cranes in the 
    Containment and Auxiliary Buildings, and deletion of statements in 
    the bases of TS 2.8 pertaining to crane interlocks does not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated. Specifications 2.8(8), 2.11 and the 
    deleted statements in the bases of Specification 2.8 need not be 
    retained in the TS based upon Criteria 1 through 4 of the ``Final 
    Policy Statement on Technical Specifications Improvements for 
    Nuclear Power Reactors,'' dated July 22, 1993 (58 FR 39132).
        Controls and limitations for the operation and testing of these 
    cranes and interlocks will be incorporated into the Updated Safety 
    Analysis Report (USAR). The requirements of TS 2.8(8) and 
    restrictions of TS 2.11 are currently contained in Station 
    procedures to ensure that the handling of fuel assemblies, control 
    element assemblies (CEAs) and heavy loads is accomplished safely and 
    effectively. These revisions make the FCS Technical Specifications 
    more similar to Standard Technical Specifications (STS), which do 
    not contain requirements or restrictions concerning the operation of 
    fuel handling cranes or overhead cranes.
        The revision proposed for TS 3.2, Table 3-5, Item 1 will make 
    its surveillance frequency identical to the frequency specified in 
    STS 3.1.5.7. The proposed frequency will require testing CEA drop 
    times prior to reactor criticality after each removal of the reactor 
    vessel closure head, which is the most appropriate time to perform 
    the surveillance. The proposed frequency will ensure that the CEAs 
    drop into the core within the time specified in the safety analysis 
    and, therefore, does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed deletion of TS 3.2, Table 3-5, Item 5, which 
    currently requires testing refueling system interlocks prior to the 
    refueling outage does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    Table 3-5, Item 5, does not need to be retained in the TS based upon 
    Criteria 1 through 4 of the ``Final Policy Statement on Technical 
    Specifications Improvements for Nuclear Power Reactors,'' dated July 
    22, 1993. Controls and limitations for testing the refueling system 
    interlocks will be incorporated into the USAR. The requirements for 
    testing refueling system interlocks are already contained in Station 
    procedures. This revision makes the FCS Technical Specifications 
    more similar to STS, which do not contain requirements or 
    restrictions pertaining to testing refueling system interlocks.
        The proposed revision to TS 3.2, Table 3-5, Item 10, ensures 
    consistent use of terminology among the frequencies specified in 
    Table 3-5. The proposed revision clarifies the wording and 
    introduces additional operational flexibility such that the 
    surveillance could be performed before 720 hours of system 
    operation, if warranted by plant conditions or beneficial to plant 
    operation. Therefore, the proposed revision does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The remaining TS revisions are administrative in nature in that 
    they correct references, titles, misspelling(s), and page numbers, 
    or revise wording to be consistent with defined intervals within the 
    TS. Therefore, they do not increase the probability or consequences 
    of an accident previously evaluated. None of the proposed TS 
    revisions will impact the function or method of operation of plant 
    systems, structures, or components.
        (2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed revisions to TS 5.5 and 5.8 which delete the review 
    and/or audit of the emergency, site security and safeguards 
    contingency plans and implementing procedures from the TS are 
    administrative in nature and in accordance with the guidance of GL 
    93-07. The proposed revisions will not affect the operation of any 
    system, structure, or component and therefore do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed revision to TS 2.5 will still require a backup 
    supply of water for the emergency feedwater storage tank to be 
    available. However, several other available sources of water are 
    preferred over river water, such as, the water plant demineralized 
    water system and the outside condensate storage tank. Therefore, the 
    proposed revision does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed deletion of TS 2.8(8) pertaining to fuel handling 
    cranes, deletion of TS 2.11 pertaining to overhead cranes in the 
    Containment and Auxiliary Buildings and deletion of statements in 
    the bases of TS 2.8 pertaining to crane interlocks does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated. Specifications 2.8(8), 2.11 and the 
    deleted statements in the bases of Specification 2.8 need not be 
    retained in the TS based upon Criteria 1 through 4 of the ``Final 
    Policy Statement on Technical Specifications Improvements for 
    Nuclear Power Reactors,'' dated July 22, 1993.
        The requirements of TS 2.8(8) and restrictions of TS 2.11 are 
    currently contained in Station procedures to ensure that the 
    handling of fuel assemblies, CEAs and heavy loads is accomplished 
    safely and effectively. These revisions make the FCS Technical 
    Specifications more similar to STS, which do not contain 
    requirements or restrictions concerning the operation of fuel 
    handling cranes or overhead cranes.
        The proposed revision to TS 3.2, Table 3-5, Item 1, is an 
    administrative revision to the frequency of CEA drop time testing. 
    The proposed frequency is the most appropriate time to perform the 
    surveillance to ensure that the CEAs drop into the core within the 
    time specified in safety analysis and is identical to the frequency 
    specified in STS 3.1.5.7. Therefore, the proposed revision does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        The proposed deletion of TS 3.2, Table 3-5, Item 5, which 
    currently requires testing the refueling system interlocks prior to 
    the refueling outage, does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    Table 3-5, Item 5, does not need to be retained in the TS based upon 
    Criteria 1 through 4 of the ``Final Policy Statement on Technical 
    Specifications Improvements for Nuclear Power Reactors,'' dated July 
    22, 1993. The requirements for testing refueling 
    [[Page 18628]] system interlocks are currently contained in Station 
    procedures. This revision makes the FCS Technical Specifications 
    more similar to STS, which do not contain requirements or 
    restrictions pertaining to testing refueling system interlocks.
        The proposed revision to TS 3.2, Table 3-5, Item 10, ensures 
    consistent use of terminology among the frequencies specified in 
    Table 3-5. The proposed revision clarifies the wording and 
    introduces additional operational flexibility such that the 
    surveillance could be performed before 720 hours of system 
    operation, if warranted by plant conditions or beneficial to plant 
    operation. Therefore, the proposed revision does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The remaining TS revisions are administrative in nature in that 
    they correct references, titles, misspelling(s), and page numbers, 
    or revise wording to be consistent with defined intervals within the 
    TS. Therefore, they do not create the possibility of a new or 
    different kind of accident.
        (3) The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed revisions to TS 5.5 and 5.8 concerning the review 
    and/or audit of the emergency, site security and safeguards 
    contingency plans and implementing procedures do not involve a 
    significant reduction in a margin of safety. The audit and review 
    processes are administrative functions which will be retained 
    outside the TS in a manner that fully satisfies regulatory 
    requirements.
        Removing the requirement of TS 2.5 that Missouri River water 
    from the fire water system shall be available to provide a backup 
    water supply to the emergency feedwater storage tank improves 
    operational flexibility without reducing any safety margins. Better 
    sources of backup water are available to replenish the emergency 
    feedwater storage tank. Although deleted from TS 2.5, the fire water 
    system is still required to be available to meet the requirements of 
    paragraph 3.F of the FCS Operating License. Therefore, the proposed 
    revision does not involve a significant reduction in a margin of 
    safety.
        The proposed deletion of TS 2.8(8) pertaining to fuel handling 
    cranes, deletion of TS 2.11 pertaining to overhead cranes in the 
    Containment and Auxiliary Buildings and deletion of statements in 
    the bases of TS 2.8 pertaining to crane interlocks does not involve 
    a significant reduction in a margin of safety. Specifications 
    2.8(8), 2.11 and the deleted statements in the bases of 
    Specification 2.8 do not need to be retained in the TS based upon 
    Criteria 1 through 4 of the ``Final Policy Statement on Technical 
    Specifications Improvements for Nuclear Power Reactors,'' dated July 
    22, 1993.
        The requirements of Specification 2.8(8) and restrictions of 
    Specification 2.11 are currently contained in Station procedures to 
    ensure that the handling of fuel assemblies, CEAs and heavy loads is 
    accomplished safely and effectively. These revisions make the FCS 
    Technical Specifications more similar to STS, which do not contain 
    requirements or restrictions concerning the operation of fuel 
    handling cranes or overhead cranes.
        The proposed revision to TS 3.2, Table 3-5, Item 1, is an 
    administrative revision to the frequency of CEA drop time testing. 
    The proposed frequency is the most appropriate time to perform the 
    surveillance to ensure that the CEAs drop into the core within the 
    time specified in the safety analysis and is identical to the 
    frequency specified in STS 3.1.5.7. Therefore, the proposed revision 
    does not involve a significant reduction in a margin of safety.
        The proposed deletion of TS 3.2, Table 3-5, Item 5, which 
    currently requires testing the refueling system interlocks prior to 
    the refueling outage does not involve a significant reduction in a 
    margin of safety. Table 3-5, Item 5, does not need to be retained in 
    the TS based upon Criteria 1 through 4 of the ``Final Policy 
    Statement on Technical Specifications Improvements for Nuclear Power 
    Reactors,'' dated July 22, 1993. The requirements for testing 
    refueling system interlocks are currently contained in Station 
    procedures. This revision makes the FCS Technical Specifications 
    more similar to STS, which do not contain requirements or 
    restrictions pertaining to testing refueling system interlocks.
        The proposed revision to TS 3.2, Table 3-5, Item 10, ensures 
    consistent use of terminology among the frequencies specified in 
    Table 3-5. The proposed revision clarifies the wording and 
    introduces additional operational flexibility such that the 
    surveillance could be performed before 720 hours of system operation 
    if warranted by plant conditions or beneficial to plant operation. 
    Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        The remaining TS revisions are administrative in nature in that 
    they correct references, titles, misspelling(s), and page numbers, 
    or revise wording to be consistent with defined intervals within the 
    TS. Therefore, they do not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: LeBoeuf, Lamb, Leiby, and MacRae, 1875 
    Connecticut Avenue, NW., Washington, DC 20009-5728
        NRC Project Director: William H. Bateman
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama
    
        Date of amendments request: March 6, 1995
        Description of amendments request: The proposed amendment would 
    relocate the seismic and meteorological monitoring instrumentation from 
    the Technical Specifications to the Final Safety Analysis Report in 
    accordance with the ``Final Policy Statement on Technical 
    Specifications Improvements for Nuclear Power Reactors,'' dated July 
    22, 1993.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No. The proposed change relocates information from the TS to the 
    FSAR and has no impact on physical plant operation or configuration. 
    The continued capability of the seismic and meteorological 
    instrumentation to perform its intended function will be ensured 
    through controlled change processes governed by 10 CFR 50.59.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        No. The sole function of the seismic and meteorological 
    monitoring instrumentation is to record data. The proposed change 
    will not involve any design change or modification to the plant. The 
    proposed change will not alter the operation of the plant or the 
    manner in which it is operated. Any subsequent change to the Seismic 
    and Meteorological Monitoring Instrumentation requirements will 
    undergo a review in accordance with the criteria of 10 CFR 50.59 to 
    endure that the change does not involve an unreviewed safety 
    question.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the proposed change involve a significant reduction in a 
    margin of safety?
        No. The proposed change will relocate Seismic and Meteorological 
    Monitoring Instrumentation requirements from the TS to licensee 
    controlled documents subject to the criteria of 10 CFR 50.59. The 
    proposed change will have no adverse impact on any protective 
    boundary or safety limit.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial 
    [[Page 18629]] Library, 212 W. Burdeshaw Street, Post Office Box 1369, 
    Dothan, Alabama 36302
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: William H. Bateman
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: November 15, 1994; superseded March 7, 
    1995 (TS 94-12).
        Description of amendment request: The proposed change would remove 
    the frequency for each of the audits specified in the administrative 
    controls section of the technical specifications (TS), except those 
    related to the fire protection system. The requirements to perform the 
    audits would be retained, but the frequency for their performance would 
    be controlled by a requirement to be added to the Nuclear Quality 
    Assurance Plan. This would require that the audits listed in the TS 
    (except those related to the fire protection system) be performed on a 
    biennial frequency. In addition, the proposed change would remove the 
    requirement to perform site Radiological Emergency Plan, Physical 
    Security Plan, and the Safeguard Contingency Plan reviews and audits 
    from the TS, since these requirements presently exist in their 
    respective Plans.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The standards used to arrive at a determination that a Technical 
    Specification change request involves no significant hazards 
    consideration are included in the Commission's regulations, 10 CFR 
    50.92, which states that no significant hazards considerations are 
    involved if the operation of the facility in accordance with the 
    proposed amendment would not: (1) involve a significant increase in 
    the probability or consequences of an accident previously evaluated; 
    or (2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or (3) involve a significant 
    reduction in a margin of safety. Each standard is addressed as 
    follows:
        1. Operation of the facility in accordance with the proposed 
    technical specifications would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The likelihood that an accident will occur is neither increased 
    or decreased by the Technical Specification change which only 
    affects review and audit frequencies. This Technical Specification 
    change will not impact the function or method of operation of plant 
    equipment. Thus, there is not a significant increase in the 
    probability of a previously analyzed accident due to this change. No 
    systems, equipment, or components are affected by the proposed 
    changes. Thus, the consequences of a malfunction of equipment 
    important to safety previously evaluated in the FSAR are not 
    increased by this change.
        The proposed change only affects review and audit frequencies. 
    As such, the proposed change has no impact on accident initiators or 
    plant equipment, and thus, does not affect the probabilities or 
    consequences of an accident.
        Therefore, we conclude that this change does not significantly 
    increase the probabilities or consequences of an accident.
        2. Operation of the facility in accordance with the proposed 
    technical specifications would not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not involve changes to the physical 
    plant or operations. Since program audits do not contribute to 
    accident initiation, a change related to audit functions cannot 
    produce a new accident scenario or produce a new type of equipment 
    malfunction. Also, this change does not alter any existing accident 
    scenarios. The proposed change does not affect equipment or its 
    operation, and, thus, does not create the possibility of a new or 
    different kind of accident. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident.
        3. Operation of the facility in accordance with the proposed 
    technical specifications would not involve a significant reduction 
    in a margin of safety.
        The proposed change concerning conduct of reviews and audits 
    does not directly affect plant equipment or operation. Safety limits 
    and limiting safety system settings are not affected by this 
    proposed change.
        Therefore, use of the proposed Technical Specification would not 
    involve any reduction in the margin of safety.
        The NRC has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: March 2, 1995
        Description of amendment request: The proposed changes would revise 
    Technical Specification 4.6.1.2.a to reference the testing requirements 
    of 10 CFR Part 50, Appendix J, and to state that the Nuclear Regulatory 
    Commission-approved exemptions to the applicable regulatory 
    requirements are permitted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A discussion of these standards as they relate to this ... 
    amendment request follows.
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The proposed change ... revises the North Anna Units 1 and 2 
    Technical Specification Surveillance Requirement 4.6.1.2.a to 
    reference the testing frequency requirements of 10 CFR 50 Appendix J 
    and to state that NRC approved exemptions to the applicable 
    regulatory requirements are permitted. The current Technical 
    Specification requires Type A tests be conducted in accordance with 
    Appendix J to 10 CFR 50. The proposed administrative change simply 
    includes the statement ``as modified by NRC-approved exemptions.'' 
    No new requirements are added, nor are any existing requirements 
    deleted. Any specific changes to the requirements of Appendix J will 
    require a submittal from Virginia Electric and Power Company under 
    10 CFR 50.12 and subsequent review and approval by the NRC prior to 
    implementation. The proposed change is stated generically to avoid 
    the need for further Technical Specification changes if different 
    exemptions are approved in the future.
        The proposed change, in itself, does not affect reactor 
    operations or accident analyses and has no radiological 
    consequences. The change provides clarification so that future 
    Technical Specifications changes will not be necessary to correspond 
    to applicable NRC-approved exemptions from the requirements of 
    Appendix J. This exemption request is consistent with the intent of 
    the regulation.
        Therefore, this proposed change does not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The proposed Technical Specification amendment for Units 1 and 2 
    provides clarification to a specification that paraphrases a 
    codified requirement.
        Since the ... proposed Technical Specifications change would not 
    change the [[Page 18630]] design, configuration, or method of 
    operation of the plant, the changes would not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The proposed North Anna Units 1 and 2 Technical Specifications 
    change is administrative and clarifies the relationship between the 
    requirements of Technical Specification Surveillance Requirement 
    4.6.1.2.a, Appendix J, and any approved exemptions to Appendix J. It 
    does not, in itself, change a Safety Limit or a Limiting Condition 
    for Operation. The NRC will directly approve any proposed change or 
    exemption to Appendix J prior to implementation.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: November 10, 1994
        Description of amendment request: The proposed amendment request 
    will clarify the surveillance requirements for the reactor protection 
    and the engineered safeguards system instrumentation and actuation 
    logic.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of Surry Power Station in accordance with the proposed 
    Technical Specifications change will not:
        1. Involve a significant increase in the probability of 
    occurrence or consequences of an accident previously evaluated.
        The proposed change to clarify the surveillance requirements for 
    the Reactor Protection and Engineered Safeguards Systems 
    instrumentation and actuation logic has no impact on the probability 
    of an accident occurrence. The instrumentation and actuation logic 
    will continue to be operated in the same manner. The actual test 
    frequency is not changing. Rather, surveillance requirements are 
    being clarified to represent the actual testing and the licensing 
    and design bases. Testing of these instruments and actuation logic 
    are presently design limited and would otherwise require using 
    temporary modifications to complete the testing. Since the testing 
    is not changing, the clarification of the actual testing does not 
    contribute to the probability of any previously analyzed accident. 
    The Reactor Protection and Engineered Safeguards Systems 
    instrumentation and actuation logic will be operated in the same 
    manner and the system operability requirements are not being 
    altered. Therefore, the consequences of any design basis accident 
    are not being increased by the proposed change to clarify the 
    surveillance test requirements for the Reactor Protection and 
    Engineered Safeguards System instrumentation and actuation logic.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        There are no plant modifications or changes in methods of plant 
    operation introduced by this change in the clarification of the 
    testing for the Reactor Protection and Engineered Safeguards Systems 
    instrumentation and actuation logic. The plant is not being operated 
    or tested in a different manner due to the proposed change. 
    Therefore, no new accidents or accident precursors are generated by 
    the proposed change to clarify the surveillance test requirements.
        Clarifying the surveillance test requirements to represent the 
    original licensing design basis and test conditions does not create 
    the possibility of a new or different accident than previously 
    analyzed.
        3.Involve a significant reduction in a margin of safety.
        Clarification of the testing for the Reactor Protection and 
    Engineered Safeguards Systems instrumentation and actuation logic 
    surveillance requirements does not affect the margin of safety in 
    that the operability requirements for these safety systems remain 
    unchanged. The existing testing is performed in accordance with 
    plant design and licensing basis and provides adequate indication of 
    the operability of the affected instrumentation or actuation logic. 
    The Reactor Protection and Engineered Safeguards Systems 
    instrumentation and actuation logic are fully tested on a refueling 
    cycle basis which includes complete operation of each relay and end 
    device. Therefore, the margin of safety is not altered by the 
    proposed clarification of the testing for the Reactor Protection and 
    Engineered Safeguards Systems instrumentation and actuation logic.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: November 22, 1994
        Description of amendment request: The proposed amendment request 
    would delete unnecessary descriptive phrases regarding the number of 
    cells in the station and emergency diesel generator batteries.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The deletion of the descriptive references regarding the number 
    of cells in the station and emergency diesel generator batteries is 
    an administrative change and therefore does not:
        1. Involve an increase in the probability of occurrence or 
    consequences of an accident previously evaluated.
        The proposed change to delete the descriptive references 
    associated with the station and emergency diesel generator batteries 
    (60 cell or 56 cell, respectively) has no impact on the probability 
    of an accident occurrence. The change is administrative in nature 
    and therefore does not affect the operation of the units. The 
    batteries will continue to be operated in the same manner as before 
    the change with operability based on design voltage and capacity 
    requirements necessary to ensure safety functions can be performed. 
    Prescribed surveillance testing will continue to ensure the 
    operability of individual battery cells. Consequently, the proposed 
    change does not contribute to the probability of occurrence or 
    consequences of any design basis accident.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        This is an administrative change to delete the descriptive 
    references associated with the station and emergency diesel 
    generator batteries. There are no plant modifications being 
    implemented by the proposed change and plant operations are not 
    being changed. Provided the required design voltage and capacity are 
    maintained, the batteries remain fully operable and capable of 
    performing their intended safety functions. Individual battery cell 
    surveillance requirements remain unchanged. Therefore, no new 
    accidents or accident precursors are created by the proposed change.
        3. Involve a reduction in a margin of safety as defined in the 
    Technical Specifications. [[Page 18631]] 
        The proposed administrative change to delete the descriptive 
    references associated with the station and emergency diesel 
    generator batteries (60 cell or 56 cell, respectively) is 
    administrative in nature. Provided the required design voltage and 
    capacity are maintained, the batteries remain fully operable and 
    capable of performing their intended safety functions as assumed in 
    the safety analyses. Individual battery cell surveillance 
    requirements remain unchanged. Therefore, the analyzed margin of 
    safety is not reduced by the proposed change.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: January 24, 1995
        Description of amendment request: The proposed amendment request 
    would increase the current Technical Specification pressurizer safety 
    valve lift setpoint acceptance criterion from plus or minus 1% as-found 
    and plus or minus 1% as-left to plus or minus 3% as-found and plus or 
    minus 1% as-left.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed Technical Specifications change does not involve a 
    significant hazards consideration because operation of Surry Units 1 
    and 2 in accordance with this change would not:
        a. involve a significant increase in the probability or 
    consequences of an accident previously evaluated. Affected safety-
    related parameters were analyzed for a change to Surry Units 1 and 2 
    Technical Specification 3.1.A.3.b. It was determined that the 
    primary and secondary side overpressure safety limits would not be 
    exceeded in the most limiting overpressure transient (Loss of Load, 
    Locker Rotor, and Rod Withdrawal events) with the pressurizer safety 
    valve lift setpoint acceptance criterion increased to [plus or 
    minus] 3%. The DNBR [departure from nucleate boiling ratio] results 
    of transients impacted by the setpoint acceptance criterion increase 
    are not affected by the proposed change. The increased setpoint 
    acceptance criterion will not result in an inadvertent opening of 
    the pressurizer safety valves. Since the proposed change involves no 
    alterations to the physical plant, the probability of occurrence of 
    an accident or malfunction of equipment important to safety 
    previously evaluated is not increased.
        b. create the possibility of a new or different kind of accident 
    from any accident previously identified. The proposed change to 
    Surry Units 1 and 2 Technical Specification 3.1.A.3.b does not 
    involve any alterations to the physical plant which would introduce 
    any new or unique operational modes or accident precursors. Only the 
    allowable tolerance about the existing setpoint will be changed.
        c. involve a significant reduction in a margin of safety. It was 
    determined that the most limiting overpressure transients do not 
    result in maximum pressures in excess of the primary and secondary 
    side overpressure limits. The DNBR results of affected transients 
    are not made more limiting by the proposed setpoint tolerance 
    increase. Therefore, the margin of safety is unchanged by the 
    proposed increase in the safety valve setpoint acceptance criterion.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: David B. Matthews
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 21, 1995
        Description of amendment request: The amendment would revise 
    Surveillance Requirement 4.6.2.1.d for the containment spray system to 
    change the surveillance interval for the performance of the air or 
    smoke test through the containment spray header from once per 5 years 
    to once per 10 years.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed reduced testing frequency of the Containment Spray 
    System nozzles does not change the way the system is operated or the 
    Containment Spray System's operability requirements. The proposed 
    change to the surveillance frequency of safety equipment has no 
    impact on the probability of an accident occurrence nor can it 
    create a new or different type of accident. NUREG-1366 concluded 
    that the corrosion of stainless steel piping is negligible during 
    the extended surveillance interval. Since the Containment Spray 
    System is maintained dry there is no additional mechanism that could 
    cause blockage of the spray nozzles. Thus, the nozzles in the 
    Containment Spray System will remain operable during the ten year 
    surveillance interval to mitigate the consequence of an accident 
    previously evaluated. No clogging or blockage of the nozzles in the 
    Containment Spray System has been discovered during the performance 
    of the five year surveillance tests. Therefore, the testing of the 
    Containment Spray System[']s nozzles at the proposed reduced 
    frequency will not increase the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed reduced frequency testing of the Containment Spray 
    System nozzles does not change the way the Containment Spray System 
    is operated. The reduced frequency of testing of the spray nozzles 
    does not change plant operation or system readiness. The reduced 
    frequency testing of the Containment Spray System nozzles does not 
    generate any new accident precursors. Therefore, the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated is not created by the proposed changes in surveillance 
    frequency of the Containment Spray System nozzles.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        Reduced testing of the Containment Spray System nozzles does not 
    change the way the system is operated or the Containment Spray 
    System's operability requirements. NUREG-1366 concluded that the 
    corrosion of stainless steel piping is negligible during the 
    extended surveillance interval. Since the Containment Spray System 
    is maintained dry there is no additional mechanism that could cause 
    blockage of the Containment Spray System nozzles. Thus, the proposed 
    reduced testing frequency is adequate to ensure spray nozzle 
    operability. The surveillance requirements do not affect the margin 
    of safety in the operability requirements of the Containment Spray 
    System remains unaltered. The existing safety analysis remains 
    bounding. Therefore no margins of safety are adversely affected by 
    this proposed change.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    [[Page 18632]] satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 24, 1995
        Description of amendment request: The proposed amendment would add 
    a new action statement to Technical Specification 3.5.1 which would 
    provide a 72-hour allowed outage time (AOT) for one accumulator to be 
    inoperable because its boron concentration did not meet the 2300-2500 
    parts per million (ppm) band. The amendment would also change the 
    current allowed outage time for other reasons of inoperability from 1 
    hour to 24 hours.
        Changes to the surveillance requirements are also proposed to 
    incorporate the guidance of Generic Letter 93-05, ``Line-Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Operation.'' These proposed changes would base the 
    operability of the accumulator on the contained water volume and cover 
    pressure and would not require verification of the boron concentration 
    after an accumulator volume increase, provided the source of the makeup 
    water is the refueling water storage tank.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed change does not involve a significant Increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The overall protection system performance will remain within the 
    bounds of the accident analysis documented in Chapter 15 of the 
    Updated Safety Analysis Report [USAR], WCAP-1096-P, and WCAP-11883 
    since no hardware changes are proposed.
        The safety injection accumulators are credited in Section 15.6.5 
    of the Updated Safety Analysis Report for large and small break LOCA 
    [loss-of-coolant accident]. There will be no effect on these 
    analyses, or any other accident analysis, since the analysis 
    assumptions are unaffected and remain the same as discussed in 
    Section 15.6.5. Design basis accidents are not assumed to occur 
    during allowed outage times covered by the Technical Specifications. 
    As such, the ECCS [emergency core cooling system] Evaluation Model 
    equipment availability assumptions made in Section 15.6.5 remain 
    valid.
        The safety injection accumulators will continue to function in a 
    manner consistent with the above analysis assumptions and the plant 
    design basis. As such, there will be no degradation in the 
    performance of nor an increase in the number of challenges to 
    equipment assumed to function during an accident situation.
        The proposed technical specifications changes do not involve any 
    hardware changes nor do they affect the probability of any event 
    initiators. There will be no change to normal plant operating 
    parameters, ESF [engineered safety features] actuation setpoints, 
    accident mitigation capabilities, accident analysis assumptions or 
    inputs. Therefore, these changes will not increase the probability 
    of an accident or malfunction.
        The corresponding increase in CDF [core damage frequency] due to 
    the proposed change to increase the AOT of the accumulators from one 
    hour to 24 hours is insignificant. Pursuant to the guidance in 
    Section 3.5 of NSAC-125, the proposed increase in AOT does not 
    ``degrade below the design basis the performance of a safety system 
    assumed to function in the accident analysis,'' nor does it 
    ``increase challenges to safety systems assumed to function in the 
    accident analysis such that safety system performance is degraded 
    below the design basis without compensating effects.'' Therefore, it 
    is concluded that these changes do not increase the probability of 
    occurrence of a malfunction of equipment important to safety.
        (2) The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    This change is administrative in nature and does not involve any 
    change to the installed plant systems or the overall operating 
    philosophy of WCGS [Wolf Creek Generating Station].
        No new accident scenarios, transient precursors, failure 
    mechanisms, or limiting single failures are introduced as a result 
    of these proposed changes. There will be no adverse effect or 
    challenges imposed on any safety-related system as a result of these 
    changes. Therefore, the possibility of a new or different type of 
    accident is not created.
        There are no changes which would cause the malfunction of 
    safety-related equipment, assumed to be operable in the accident 
    analyses, as a result of the proposed technical specification 
    changes. No new mode failure has been created and no new equipment 
    performance burdens are imposed. Therefore, the possibility of a new 
    or different malfunction of safety-related equipment is not created.
        (3) The proposed change does not involve a significant reduction 
    in the margin of safety.
        The proposed change does not involve an significant reduction in 
    a margin of safety. There will be no change to the Departure from 
    Nucleate Boiling Ratio (DNBR) Correlation Limit, the design DNBR 
    limits, or the safety analysis DNBR limits discussed in Bases 
    Section 2.1.1.
        As discussed previously, the performance of the accumulators 
    will remain within the assumptions used in the large and small break 
    LOCA analyses, as presented in USAR Section 15.6.5. Also, there will 
    be no effect on the manner in which safety limits or limiting safety 
    system settings are determined nor will there be any effect on those 
    plant systems necessary to assure the accomplishment of protection 
    functions.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice. [[Page 18633]] 
    
    Baltimore Gas and Electric Company, Docket No. 50-318, Calvert 
    Cliffs Nuclear Power Plant, Unit No. 2, Calvert County, Maryland
    
        Date of amendment request: February 24, 1995
        Brief description of amendments: The proposed amendment would 
    revise the Calvert Cliffs, Unit No. 2, Technical Specifications (TSs). 
    Specifically, TS 4.G.1.2 would reference 10 CFR Part 50, Appendix J, 
    directly, and any approved exemptions to the Type A testing frequency 
    requirements, rather than paraphrase the regulation. The proposed 
    wording is consistent with that used in NUREG-1432, ``Standard 
    Technical Specifications - Combustion Engineering Plants,'' dated 
    September 1992.Date of publication of individual notice in Federal 
    Register: March 8, 1995 (60 FR 12789)
        Expiration date of individual notice: April 7, 1995
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: February 23, 1995, as supplemented March 
    21, 1995.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications 3.8.2.1 and 3.8.3.1 to allow 
    installation of a modification to replace the battery, main and tie 
    breakers in response to an Electrical Distribution Systems Functional 
    Inspection, conducted by the NRC in July 1991. The existing breaker 
    arrangement could result in a trip of both the battery and main 
    breakers if a fault occurs on one of the 125 VDC panelboards. The 
    licensee committed to have these breakers replaced in 1995 with a 
    better coordinated design to eliminate the concern.Date of publication 
    of individual notice in Federal Register: March 8, 1995 (60 FR 12791)
        Expiration date of individual notice: April 7, 1995
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket No. 50-498, South Texas Project, Unit 1, Matagorda County, 
    Texas
    
        Date of amendment request: March 1, 1995
        Description of amendment request: The proposed amendment would 
    modify the steam generator tube plugging criteria in Technical 
    Specification 3/4.4.5, Steam Generators, and the allowable leakage for 
    Unit 1 in Technical Specification 3/4.4.6.2, Operational Leakage, and 
    the associated Bases.Date of individual notice in the Federal Register: 
    March 13, 1995 (60 FR 13478)
        Expiration date of individual notice: April 12, 1995
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket No. 50-498, South Texas Project, Unit 1, Matagorda County, 
    Texas
    
        Date of amendment request: March 1, 1995
        Description of amendment request: The proposed amendment would 
    change Technical Specification 3/4.4.5, Steam Generators, and the 
    associated Bases to allow the use of an alternate plugging criteria 
    (known in the industry as F*) on steam generator tubes that are 
    defective or degraded within certain areas within the tubesheet. Date 
    of individual notice in the Federal Register: March 13, 1995 (60 FR 
    13481)
        Expiration date of individual notice: April 12, 1995
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of amendment request: March 9, 1994
        Description of amendment request: The proposed amendment would 
    revise the Nine Mile Point Nuclear Station, Unit 2, Technical 
    Specifications (TSs). Specifically, TS 4.6.1.2.a would be modified to 
    allow the second Primary Containment Integrated Leakage Rate Test (Type 
    A) to be performed at the fifth refueling outage (RF-05) or 72 months 
    after the first Type A test instead of the fourth refueling outage (RF-
    04) as currently scheduled.
        Date of publication of individual notice in Federal Register: March 
    23, 1995 (60 FR 15310)
        Expiration date of individual notice:  April 24, 1995
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Rochester, New York
    
        Date of application for amendment: March 13, 1995
        Brief description of amendment: The proposed amendment would revise 
    Ginna Station Technical Specification (TS) 4.4.2.4.a to replace 
    specific leakage testing frequencies for containment isolation valves. 
    This TS change will support a proposed Exemption to Title 10 of the 
    Code of Federal Regulations (10 CFR) Part 50, Appendix J, Section 
    III.D.3, requested under separate cover to exempt Type C testing of 
    certain valves during a 1995 refueling outage.
        Date of publication of individual notice in Federal Register: March 
    22, 1995 (60 FR 15167)
        Expiration date of individual notice: April 21, 1995
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment [[Page 18634]] under the special circumstances 
    provision in 10 CFR 51.12(b) and has made a determination based on that 
    assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station,Plymouth County, MassachusettsDate of application for 
    amendment: November 22, 1994
    
        Brief description of amendment: The amendment revises the allowable 
    leak rate for the main steam isolation valves from the current 11.5 
    standard cubic feet per hour (scfh) for each valve, to a maximum 
    combined main steam line leak rate of 46 scfh.
        Date of issuance: March 22, 1995
        Effective date: March 22, 1995
        Amendment No.: 160
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 18, 1995 (60 FR 
    3671) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 22, 1995. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station,Plymouth County, Massachusetts
    
        Date of application for amendment: September 6, 1994, as 
    supplemented February 15, 1995.
        Brief description of amendment: This amendment revises Technical 
    Specifications (TSs) 3.7.B.1.a, 3.7.B.1.c, 3.7.B.1.e, 3.7.B.2.a, and 
    3.7.B.2.c and adds Sections 3.7.B.1.f and 3.7.B.2.e. The additional 
    section requires both trains of standby gas treatment and control room 
    high efficiency air filtration system to be operable for the initiation 
    of fuel movement. In the event either train becomes inoperable, the 
    other train must be demonstrated to be operable within 2 hours and fuel 
    handling operations may continue for 7 days with one train inoperable. 
    Additionally, this change allows one train to be defined as operable 
    without its associated emergency power supply, provided one source of 
    normal power (startup transformer or unit auxiliary power) is 
    available.
        Date of issuance: March 22, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 161
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 26, 1994 (59 FR 
    53837) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 22, 1995. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station,Plymouth County, Massachusetts
    
        Date of application for amendment: September 6, 1994
        Brief description of amendment: This amendment would reduce the 
    Reactor Pressure Setpoint at which the shutdown cooling system 
    automatically isolates. This setpoint also isolates the low pressure 
    coolant injection valves when the shutdown cooling system is in 
    operation.
        Date of issuance: March 27, 1995
        Effective date: To be implemented within 30 days following restart 
    from refueling outage 10
        Amendment No.: 162
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 26, 1994 (59 FR 
    53837) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 27, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County,North Carolina
    
        Date of application for amendments: October 28, 1994, as 
    supplemented February 16, 1995.
        Brief description of amendments: The proposed change will revise TS 
    requirements to increase the surveillance test intervals and the 
    allowable out of service times or instruments of the reactor protection 
    system, isolation actuation system, emergency core cooling system 
    actuation system, control rod withdrawal block system, control room 
    emergency ventilation system, anticipated transient without scram, 
    recirculation pump trip (RPT), end-of-cycle RPT, and the reactor core 
    isolation cooling actuation system.
        Date of issuance: March 30, 1995Effective date: March 30, 1995
        Amendment Nos.: 175 and 206
        Facility Operating License Nos. DPR-71 and DPR-62. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 7, 1994 (59 FR 
    63114) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 30, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North CarolinaDate of application for amendment: October 24, 1994, 
    as supplemented December 6, 1994.
    
        Brief description of amendment: The amendment allows the relocation 
    of TS 3/4.3.4, Turbine Overspeed Protection and associated Bases to be 
    consistent with the new Standard Technical Specifications for 
    Westinghouse plants.
        Date of issuance: March 22, 1995
        Effective date: March 22, 1995
        Amendment No. 55
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: November 23, 1994 (59 
    FR 60379) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 22, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 
    27605. [[Page 18635]] 
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IllinoisDocket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: December 22, 1992
        Brief description of amendments: These amendments add new 
    requirements to the Technical Specifications (TS) to ensure that an 
    Essential Service Water system (SX) pump and crossover path are 
    available from a shutdown unit to serve as backup to an operating unit. 
    In addition, a new TS is added to require the unit crosstie to be open, 
    or capable of being opened, from the Main Control Room, whenever 
    either, or both units are in an operating mode (MODE 1, 2, 3, or 4).
        Date of issuance: March 20, 1995
        Effective date: March 20, 1995
        Amendment Nos.: 71, 71, 62, and 62
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 3, 1993 (58 FR 
    6994) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 20, 1995. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: September 19, 1994
        Brief description of amendment: The amendment would revise 
    Technical Specification Section 4.4.A.3, Frequency of Containment 
    Integrated Leakage Rate Test, to reference 10 CFR Part 50, Appendix J, 
    as modified by approved exemptions, directly.
        Date of issuance: March 17, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment No.: 181
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8744) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 17, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    PennsylvaniaDate of application for amendments: April 23, 1990, as 
    supplemented January 21, 1992 and March 17, 1995.
    
        Brief description of amendments: These amendments revise the 
    Appendix A Technical Specifications (TSs) for Unit 1 and Unit 2 by (a) 
    deleting TS Table 3.6-1, ``Containment Penetrations,'' (b) rewording TS 
    Definition 1.8, ``Containment Integrity,'' and TSs 3.6.1.1, 3.6.1.2, 
    3.6.3.1, and 3.9.4 relating to containment integrity, containment 
    leakage, containment isolation valves, and containment building 
    penetrations respectively to account for the deletion of TS Table 3.6-
    1, and (c) correcting terminology by replacing the word ``door'' with 
    ``hatch'' in TS 3.9.4.a.
        The Unit 1 amendment also modifies TS Table 3.3-5, ``Engineered 
    Safety Features Response Times,'' by changing the feedwater isolation 
    response time to reflect total isolation times for the main feedwater 
    regulating valve and bypass feedwater regulating valve. Minor editorial 
    changes were also incorporated in TS Table 3.3-5.
        Date of issuance: March 28, 1995
        Effective date: March 28, 1995
        Amendment Nos.: 185 and 66
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 27, 1990 (55 FR 
    26283), as supplemented April 1, 1992 (57 FR 11107) The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated March 28, 1995. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location:  B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
        Date of application for amendment: June 22, 1994
        Brief description of amendment: The amendment changes Technical 
    Specification (TS) Sections 1.6, 3.2.A, 3.9.f.5 and 4.2.A which specify 
    the Shutdown Margin (SDM) requirements that ensure the reactor can be 
    made subcritical and can be maintained sufficiently subcritical to 
    preclude inadvertent criticality in any core condition. The amendment 
    also includes a definition of Shutdown Margin, TS Section 1.45. 
    Administrative changes to TS Sections 1.7 and 3.2.b.2(b) are also 
    included to simplify definitions and eliminate unnecessary notes and 
    references.
        Date of Issuance: March 21, 1995Effective date: As of the date of 
    issuance to be implemented within60 days
        Amendment No.: 178
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37072) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated March 21, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of application for amendment: February 14, 1995
        Brief description of amendment: The amendment revises Technical 
    Specification 3.8.2, ``AC Sources-Shutdown;'' 3.8.5, ``DC Sources-
    Shutdown;'' and 3.8.8, ``Inverters-Shutdown.'' The changes revise the 
    operability requirements for the Division 3 diesel generator and the 
    Division 3 and 4 batteries, battery chargers and inverters to apply 
    only when the high pressure core spray system is required to be 
    operable.
        Date of issuance: March 21, 1995
        Effective date: March 21, 1995
        Amendment No.: 99
        Facility Operating License No. NPF-62. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 17, 1995 (60 
    FR 9412) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 21, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 
    61727. [[Page 18636]] 
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of application for amendment: June 30, 1994, as supplemented 
    March 7, 1995
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.2.7.1 to add 8 check valves to Table 3.2.7.1. 
    These valves were installed to add additional protection of the low 
    pressure Core Spray system from the high pressure Reactor Coolant 
    system. Including the valves in the TSs will assure that the proper 
    surveillance testing is done to maintain a high reliability for the 
    valves to protect the Core Spray system.
        Date of issuance: March 20, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 154
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39593) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 20, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: April 22, 1994
        Brief description of amendment: The amendment deletes the 
    operability and surveillance requirements of the condenser air ejector 
    radiation monitor from the Millstone Unit 2 Technical Specification 
    Tables 3.3-12 and 4.3-12.
        Date of issuance: March 27, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment No.: 186
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27058) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 27, 1995. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: March 31, 1994 and August 5, 
    1994
        Brief description of amendment: This amendment revises: Technical 
    Specification (TS) 3.8.1.1.b.2 which maintains diesel operability for a 
    48-hour period when the fuel storage system of one or more diesel 
    generators contains less than a 7-day supply of fuel: TS 4.8.1.1.2.h.8 
    by deletion and replacement with surveillance requirement 4.8.1.1.2.k.1 
    which permits the 24-hour diesel generator endurance run to be 
    performed in any operational condition; establish surveillance 
    requirement 4.8.1.1.2.k.2 which allows the hot restart test to be 
    conducted not only after surveillance requirement 4.8.1.1.2.k.1, but 
    also after the diesel generator has operated between 4300 kw and 4400 
    kw for one hour or after any time the diesel generator operating 
    temperature has stabilized; revise TS 3.8.1.1 to eliminate the 
    requirements to start the Emergency Diesel Generator (EDG) with an 
    inoperable offsite circuit(s) of AC electrical power; add a provision 
    that eliminates required testing of remaining EDGs when one EDG is 
    inoperable due to an inoperable support system or an independently 
    testable component with no potential for common mode failure for the 
    remaining EDGs. In addition, if testing of the EDGs is required, the 
    surveillance will be performed within 16 hours instead of 24 hours as 
    currently specified; delete the requirement to perform a Loss of 
    Offsite Power (LOOP) test (Surveillance Requirement 4.8.1.1.2.h.b) 
    following the 24-hour EDG endurance run test in its place, a hot 
    restart test (no LOOP load sequencing) will be established.
        Date of issuance: March 30, 1995
        Effective date: March 30,1995
        Amendment No.: 72
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29630) and October 12, 1994 (59 FR 51625) The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    March 30, 1995. No significant hazards consideration comments received: 
    No
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    South Carolina Electric & Gas Company, South Carolina Public 
    ServiceAuthority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: October 29, 1993, as 
    supplemented on March 11, 1994, May 18, 1994, September 20, 1994, and 
    October 20, 1994.
        Brief description of amendment: The amendment changes Operating 
    License NPF-12 to delete License Conditions 2.C.13, 2.C.14, and 2.C.32.
        Date of issuance: March 29, 1995
        Effective date: March 29, 1995
        Amendment No.: 123
        Facility Operating License No. NPF-12. Amendment revises the 
    operating license.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7698) and April 28, 1994 (59 FR 22012), as corrected June 30, 1994 
    (59 FR 33795). The May 18, 1994, September 20, 1994, and October 20, 
    1994, submittals provided supplemental and clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated March 29, 1995.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: September 30, 1993, as 
    supplemented by letters dated November 16, 1993, January 18, 1995, and 
    February 2, 1995.
        Brief description of amendments: These amendments revised the 
    technical specifications to (1) divide item 7 of Tables 3.3-3, 3.3-4, 
    3.3-5, and 4.3-2 into item 7a that addresses the existing loss-of-
    voltage (LOV) function and item 7b that separately addresses the 
    degraded grid voltage (DGV) function; (2) add footnote (d) to Table 
    3.3-3 to indicate that the DGV actuation relay logic is applicable in 
    Modes 1, 2, 3, and 4 when the diesel generator circuit breaker is open; 
    (3) replace the reference to Figure 3.3-1 in item 7a of Tables 3.3-4 
    and 3.3-5 with definite voltage and time values; (4) add note 9 to 
    Table 3.3-5 to explain the response [[Page 18637]] time for an LOV 
    signal; and (5) delete Figure 3.3-1, ``Degraded Bus Voltage Trip 
    Setting,'' and the reference to this figure from Table 3.3-4.
        Date of issuance: March 17, 1995
        Effective date: Unit 2, as of the date of completion of the 
    currrent refueling outage and must be fully implemented before the 
    plant returns to power; Unit 3, as of the date of the completion of its 
    next refueling outage and must be fully implemented before the plant 
    returns to power.
        Amendment Nos.: Unit 2 - Amendment No. 118; Unit 3 - Amendment No. 
    107
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59755). The additional information contained in the November 16, 
    1993, January 18, 1995 and February 2, 1995, letters was clarifying in 
    nature, within the scope of the initial notice and did not affect the 
    NRC staff's proposed no significant hazards consideration 
    determination.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 17, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama.
    
        Date of amendments request: January 9, 1995
        Brief description of amendments: The amendments change the 
    Technical Specifications to implement recommended changes from Generic 
    Letter (GL) 93-05, ``Line Item Technical Specification Improvements to 
    Reduce Surveillance Requirements for Testing During Power Operation,'' 
    dated September 27, 1993. Specifically, the amendments implement TS 
    changes corresponding to the following GL 93-05 line-item improvement 
    issues and numbers: Control Rod Movement Test for Pressurized Water 
    Reactors (4.2.1); Radiation Monitors (5.14); Surveillance of Boron 
    Concentration in the Accumulator/Safety Injection/Core Flood Tank 
    (7.1); Containment Spray System (8.1); Hydrogen Recombiner (8.5); and 
    Special Test Exemptions (12).
        Date of issuance: March 20, 1995
        Effective date: March 20, 1995
        Amendment Nos.: 113 and 104
        Facility Operating License Nos. NPF-2 and NPF-8. Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8756) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 20, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: December 6, 1994
        Brief description of amendment: This amendment deletes Technical 
    Specification (TS) Surveillance Requirement (SR) 4.1.3.2.2 for the 
    Axial Power Shaping Rods and relaxes surveillance intervals for TS 3/
    4.1.3.1, ``Group Height - Safety and Regulating Rod Groups;'' TS 3/
    4.4.6.2, ``Operational Leakage;'' TS 3/4.5.2, ``ECCS Subsystems - Tavg 
    equal to or greater than 280 deg.F;'' TS 3/4.6.2.1, ``Containment Spray 
    System;'' and TS 3/4.10.4, ``Special Test Exceptions Shutdown Margin.'' 
    Date of issuance: March 21, 1995Effective date: March 21, 1995 and 
    implemented not later than 90 days after issuance
        Amendment No.:  196
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8757) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 21, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: December 6, 1994
        Brief description of amendment: This amendment revises Technical 
    Specification (TS) 4.0.5, ``Applicability'' and its associated Bases to 
    eliminate the need for NRC approval of relief requests prior to 
    implementation and relaxes surveillance test intervals for TS 3/
    4.1.2.3, ``Reactivity Control Systems - Makeup Pump - Shutdown; TS 3/
    4.1.2.4, ``Reactivity Control Systems - Makeup Pumps - Operating; TS 3/
    4.1.2.6, Reactivity Control Systems - Boric Acid Pump - Shutdown; and 
    TS 3/4.1.2.7, ``Reactivity Control System - Boric Acid Pumps - 
    Operating'' from monthly to quarterly. Date of issuance: March 22, 1995
        Effective date: March 22, 1995, and to be implemented within 90 
    days
        Amendment No.: 197
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8758) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 22, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: December 9, 1994, as 
    supplemented on December 22, 1994.
        Brief description of amendment: The amendment revises the Technical 
    Specification (TS) Surveillance Requirement 4.8.1.1.2f.7. The change 
    removes the requirement to perform the hot restart test within 5 
    minutes of completing the 24-hour endurance test and places that 
    requirement in a separate TS.
        Date of issuance: March 20, 1995
        Effective date: March 20, 1995, to be implemented within 30 days
        Amendment No.: 95
        Facility Operating License No. NPF-30. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6315) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 20, 1995. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251. [[Page 18638]] 
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: August 4, 1994, as supplemented 
    on March 14, 1995 and March 28, 1995.
        Brief description of amendment: The amendment replaces Technical 
    Specification (TS) 3/4.6.2.2, Spray Additive System, with a new TS 3/
    4.6.2.2 entitled Recirculation Fluid pH control (RFPC) System. The 
    associated TS Surveillance Requirements and the Bases will also be 
    revised. In addition, the Bases section for the Refueling Water Storage 
    Tank (RWST) System will be revised.
        Date of issuance: March 30, 1995
        Effective date: March 30, 1995, to be implemented within 30 days
        Amendment No.: 96
        Facility Operating License No. NPF-30. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 28, 1994 (59 
    FR 49440) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 30, 1995. The March 14, 
    1995, and March 28, 1995, letters provided supplemental information 
    that did not change the initial proposed no significant hazards 
    consideration determination. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: September 8, 1994
        Brief description of amendment: The amendment revises the Technical 
    Specification (TS) Bases Section 3/4.9 and changes Final Safety 
    Analysis Report (FSAR) Sections 9.1.3 ``Fuel Pool Cooling and 
    Cleanup,'' 9.1.4 ``Fuel Handling System'' and 15.4.6 ``Chemical and 
    Volume Control System Malfunction That Results in a Decrease in the 
    Boron Concentration in the Reactor Coolant. The changes established 
    procedural controls to address an unreviewed safety question.
        Date of issuance: March 31, 1995
        Effective date: March 31, 1995, to be implemented within 30 days
        Amendment No.: 97
        Facility Operating License No. NPF-30. Amendment revises the 
    Technical Specification Bases and FSAR.
        Date of initial notice in Federal Register: March 1, 1995 (60 FR 
    11151) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 31, 1995. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: December 8, 1994, as 
    supplemented by letter dated February 16, 1995.
        Brief description of amendment: The proposed amendment would change 
    Standby Gas Treatment Power Supply Requirements during refueling 
    operations.
        Date of issuance: March 23, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 30 days
        Amendment No.: 143
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 15, 1995 (60 
    FR 8759) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 23, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, Vermont 05301.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: October 31, 1994
        Brief description of amendment: The amendment relocated 
    requirements regarding safety/relief valve position indication 
    instrumentation from the Technical Specifications to other licensee-
    controlled documents.
        Date of issuance: March 27, 1995
        Effective date: March 27, 1995, to be implemented prior to restart 
    from the spring 1995 refueling outage
        Amendment No.: 135
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65831) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 27, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    NuclearPower Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: December 2, 1994
        Brief description of amendment: The amendment revises Kewaunee 
    Nuclear Power Plant (KNPP) Technical Specification (TS) 3.2 by deleting 
    the requirements for the charging pumps, high concentration boric acid 
    in the boric acid storage tanks (BASTs), the boric acid transfer pumps, 
    and boric acid heat tracing. Changes to TS 3.3 and Table TS 3.5.3 add 
    requirements associated with the emergency core cooling system (ECCS) 
    accumulators, remove the requirements associated with the boric acid 
    storage tanks and increase the minimum required boron concentration in 
    the refueling water storage tank (RWST). Additionally, the surveillance 
    requirements involving the BASTs, associated valves and heat tracing 
    located in Table TS 4.1-1, Table TS 4.1-2 and Section 4.5 have been 
    deleted.
        Date of issuance: March 28, 1995
        Effective date: March 28, 1995, to be implemented within 20 days
        Amendment No.: 116
        Facility Operating License No. DPR-43. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    508). The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 28, 1995. No significant hazards 
    consideration comments received: None.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
    
    Notice Of Issuance Of Amendments To Facility Operating LicensesAnd 
    Final Determination Of No Significant Hazards ConsiderationAnd 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    [[Page 18639]] and regulations. The Commission has made appropriate 
    findings as required by the Act and the Commission's rules and 
    regulations in 10 CFR Chapter I, which are set forth in the license 
    amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By May 12, 1995, the licensee 
    may file a request for a hearing with respect to issuance of the 
    amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to [[Page 18640]] participate fully in the 
    conduct of the hearing, including the opportunity to present evidence 
    and cross-examine witnesses. Since the Commission has made a final 
    determination that the amendment involves no significant hazards 
    consideration, if a hearing is requested, it will not stay the 
    effectiveness of the amendment. Any hearing held would take place while 
    the amendment is in effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Northeast Nuclear Energy Company, Docket No. 50-245, 
    MillstoneNuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of application for amendment: March 17, 1995
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) Surveillance Requirement 4.7.D.1.c.1 by replacing 
    the once per quarter stroke test for containment isolation valves 
    (CIVs) with the requirement that the CIVs be tested in accordance with 
    the inservice testing program. In addition, there are some editorial 
    changes, minor renumbering of subsections, to reflect the TS revisions.
        Date of issuance: March 21, 1995
        Effective date: As of the date of issuance to be implemented 
    immediately
        Amendment No.: 81
        Facility Operating License No. DPR-21. Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated March 21, 1995.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: Phillip F. McKee
        Dated at Rockville, Maryland, this 5th day of April, 1995.
        For the Nuclear Regulatory Commission
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects - III/IV, Office of 
    Nuclear Reactor Regulation
    [Doc. 95-8845 Filed 4-11-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
04/12/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-8845
Dates:
March 22, 1995
Pages:
18621-18640 (20 pages)
PDF File:
95-8845.pdf