97-10326. Notice of Amendment to Certificate of Compliance GDP-1 for the U.S. Enrichment Corporation, Paducah Gaseous Diffusion Plant, Paducah, KY  

  • [Federal Register Volume 62, Number 77 (Tuesday, April 22, 1997)]
    [Notices]
    [Pages 19631-19632]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-10326]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket 70-7001]
    
    
    Notice of Amendment to Certificate of Compliance GDP-1 for the 
    U.S. Enrichment Corporation, Paducah Gaseous Diffusion Plant, Paducah, 
    KY
    
        The Director, Office of Nuclear Material Safety and Safeguards, has 
    made a determination that the following amendment request is not 
    significant in accordance with 10 CFR 76.45. In making that 
    determination, the staff concluded that: (1) There is no change in the 
    types or significant increase in the amounts of any effluents that may 
    be released offsite; (2) there is no significant increase in individual 
    or cumulative occupational radiation exposure; (3) there is no 
    significant construction impact; (4) there is no significant increase 
    in the potential for, or radiological or chemical consequences from, 
    previously analyzed accidents; (5) the proposed changes do not result 
    in the possibility of a new or different kind of accident; (6) there is 
    no significant reduction in any margin of safety; and (7) the proposed 
    changes will not result in an overall decrease in the effectiveness of 
    the plant's safety, safeguards or security programs. The basis for this 
    determination for the amendment request is shown below.
        The NRC staff has reviewed the certificate amendment application 
    and concluded that it provides reasonable assurance of adequate safety, 
    safeguards, and security, and compliance with NRC requirements. 
    Therefore, the Director, Office of Nuclear Material Safety and 
    Safeguards, is prepared to issue an amendment to the Certificate of 
    Compliance for the Paducah Gaseous Diffusion Plant. The staff has 
    prepared a Compliance Evaluation Report which provides details of the 
    staff's evaluation.
        The NRC staff has determined that this amendment satisfies the 
    criteria for a categorical exclusion in accordance with 10 CFR 51.22. 
    Therefore, pursuant to 10 CFR 51.22(b), no environmental impact 
    statement or environmental assessment need be prepared for this 
    amendment.
        USEC or any person whose interest may be affected may file a 
    petition, not exceeding 30 pages, requesting review of the Director's 
    Decision. The petition must be filed with the Commission not later than 
    15 days after publication of this Federal Register Notice. A petition 
    for review of the Director's Decision shall set forth with 
    particularity the interest of the petitioner and how that interest may 
    be affected by the results of the Decision. The petition should 
    specifically explain the reasons why review of the Decision should be 
    permitted with particular reference to the following factors: (1) The 
    interest of the petitioner; (2) how that interest may be affected by 
    the Decision, including the reasons why the petitioner should be 
    permitted a review of the Decision; and (3) the petitioner's areas of 
    concern about the activity that is the subject matter of the Decision. 
    Any person described in this paragraph (USEC or any person who filed a 
    petition) may file a response to any petition for review, not to exceed 
    30 pages, within 10 days after filing of the petition. If no petition 
    is received within the designated 15-day period, the Director will 
    issue the final amendment to the Certificate of Compliance without 
    further delay. If a petition for review is received, the Decision on 
    the amendment application will become final in 60 days, unless the 
    Commission grants the petition for review or otherwise acts within 60 
    days after publication of this Federal Register Notice.
        A petition for review must be filed with the Secretary of the 
    Commission, U.S. Nuclear Regulatory Commission, Washington, DC 20555-
    0001, Attention: Docketing and Services Branch, or may be delivered to 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW, Washington, DC, by the above date.
        For further details with respect to the action see (1) the 
    application for amendment and (2) the Commission's Compliance 
    Evaluation Report. These items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW, Washington, DC, and at the Local Public Document Room.
        Date of amendment request: December 23, 1996.
        Brief description of amendment: The amendment changes the Technical 
    Safety Requirement surveillance for the
    
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    Autoclave High Pressure Systems to reflect the ability to test all 
    inner and outer penetration isolation valves.
    
    Basis for Finding of No Significance
    
        1. The proposed amendment will not result in a change in the types 
    or significant increase in the amounts of any effluents that may be 
    released offsite.
        The proposed TSR changes reflect the autoclave piping modifications 
    that permit independent testing of the inner and outer penetration 
    isolation valves. Testing of these valves demonstrates the ability to 
    establish containment in the event of uranium hexafluoride leakage from 
    the cylinder into the autoclave. The proposed changes provide enhanced 
    assurance that the containment function will be available if needed. 
    These changes have no impact on plant effluents and will not result in 
    any impact to the environment.
        2. The proposed amendment will not result in a significant increase 
    in individual or cumulative occupational radiation exposure.
        The proposed changes provide enhanced assurance that the autoclave 
    containment function will be available if needed. The changes will not 
    result in increased individual or cumulative occupational radiation 
    exposure.
        3. The proposed amendment will not result in a significant 
    construction impact.
        The proposed changes will not result in any building construction, 
    therefore, there will be no construction impacts.
        4. The proposed amendment will not result in a significant increase 
    in the potential for, or radiological or chemical consequences from, 
    previously analyzed accidents.
        The proposed changes allow testing of the inner and outer 
    penetration isolation valves. This testing of the autoclave containment 
    function is not involved in any precursor to an evaluated event; 
    therefore, the potential of occurrence of an evaluated event is 
    unaffected. The proposed changes provide enhanced assurance that the 
    function will be available if required; the consequences of previously 
    evaluated accidents are not increased.
        5. The proposed amendment will not result in the possibility of a 
    new or different kind of accident.
        The autoclave piping configuration modifications permit independent 
    testing of the inner and outer penetration isolation valves to 
    demonstrate the ability to establish containment in the event of a leak 
    from the cylinder into the autoclave. The changes affect only the 
    autoclave isolation valves and create no new operating conditions or 
    new plant configuration that could lead to a new or different type of 
    accident.
        6. The proposed amendment will not result in a significant 
    reduction in any margin of safety.
        The proposed changes reflect modifications that permit independent 
    testing of the inner and outer penetration isolation valves. The 
    proposed changes enhance the availability of the autoclave containment 
    function. There is no reduction in the margin of safety.
        7. The proposed amendment will not result in an overall decrease in 
    the effectiveness of the plant's safety, safeguards or security 
    programs.
        The proposed changes reflect the autoclave piping configuration 
    modifications made to permit independent testing of inner and outer 
    penetration isolation valves. Testing of these valves demonstrates the 
    ability to establish containment in the event of uranium hexafluoride 
    leakage from the cylinder into the autoclave. The changes do not affect 
    any other equipment functions or administrative requirements. The 
    testing of the autoclave containment function is not addressed in the 
    safeguards and security programs. The effectiveness of the safety, 
    safeguards, and security programs is not decreased.
        Effective date: June 23, 1997.
        Certificate of Compliance No. GDP-1: Amendment will revise the 
    Technical Safety Requirements.
        Local Public Document Room location: Paducah Public Library, 555 
    Washington Street, Paducah, Kentucky 42003.
    
        Dated at Rockville, Maryland, this 14th day of April 1997.
    
        For the Nuclear Regulatory Commission.
    Carl J. Paperiello,
    Director, Office of Nuclear Material Safety and Safeguards.
    [FR Doc. 97-10326 Filed 4-21-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
04/22/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-10326
Dates:
June 23, 1997.
Pages:
19631-19632 (2 pages)
Docket Numbers:
Docket 70-7001
PDF File:
97-10326.pdf