X97-10423. Biweekly Notice  

  • [Federal Register Volume 62, Number 78 (Wednesday, April 23, 1997)]
    [Notices]
    [Pages 19825-19845]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X97-10423]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 29, 1997, through April 11, 1997. The 
    last biweekly notice was published on April 9, 1997 (62 FR 17223).
    
    Notice of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunith For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By May 23, 1997, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with
    
    [[Page 19826]]
    
    the applicant on a material issue of law or fact. Contentions shall be 
    limited to matters within the scope of the amendment under 
    consideration. The contention must be one which, if proven, would 
    entitle the petitioner to relief. A petitioner who fails to file such a 
    supplement which satisfies these requirements with respect to at least 
    one contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: March 17, 1997
        Description of amendment request: The proposed change would revise 
    eight specifications for 18-month tests to delete a conditional 
    statement that the testing be done while the unit is shut down and to 
    clarify that Harris Nuclear Plant (HNP) may take credit for tests on 
    some components which are performed while the unit is at power.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed changes permit HNP to evaluate the conditions 
    required to safely perform a test, but the changes do not directly 
    affect the functioning or operation of any plant equipment. Since no 
    equipment operation is involved there is no increase in the 
    probability or consequence of any previously identified accident.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the conditional statements on the 
    surveillance frequencies do not involve any physical alterations or 
    additions to plant equipment or alter the manner in which any 
    safety-related system performs itsfunction or is operated. 
    Therefore, the proposed change does not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed changes to the conditional statements on the 
    surveillance frequency allows HNP to evaluate the conditions needed 
    to safely perform the required testing. There is no change in the 
    frequency of testing or in the testing which is required. There is 
    no change in the responsibility of HNP toperform tests in a safe and 
    responsible manner, and any changes to procedures will have to be 
    individually evaluated to ensure that they do not reduce the margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Mark Reinhart, Acting
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: January 30, 1997
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 1.0, ``Definitions;'' TS 3/4.6.1, 
    ``Primary Containment'' and associated Bases; and TS 5.4.2, ``Reactor 
    Coolant System Volume'' for Byron and Braidwood to support steam 
    generator replacement. ComEd will be replacing the original 
    Westinghouse D4 steam generators at Byron and Braidwood with Babcock 
    and Wilcox International steam generators. The replacement steam 
    generators increase the Reactor Coolant System volume which results in 
    a higher calculated peak containment pressure (Pa) value.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Each of the [replacement steam generators] RSGs has a larger 
    [reactor coolant system] RCS side volume than the original steam 
    generators (OSGs). As a result of the RCS
    
    [[Page 19827]]
    
    volume increase, the mass and energy release during the blowdown 
    phase of the large break loss of coolant accident (LBLOCA) is 
    increased. Additionally, the heat transfer rate of the RSGs is 
    greater than the OSGs, and the RSGs will operate at a slightly 
    higher pressure than that for the OSGs. Consequently, the steam 
    enthalphy exiting the break during the reflood period, with the RSG, 
    will be greater than that for the OSG. This results in an increase 
    in the containment building peak pressure, Pa.
        The proposed revisions to the Technical Specifications involve 
    the specified value of Unit 1 RCS volume and the defined value of 
    Unit 1 Pa. Several editorial changes are also being made 
    to improve clarity and consistency of the TS.
        RCS volume is not an initiator for any event and an increase in 
    volume does not affect any operating margin or requirements. 
    Therefore, increasing the primary volume does not increase the 
    probability of any event previously analyzed.
        The revised value of Pa continues to be less than the 
    design basis pressure for the containment building structure. The 
    change represents only a revision to the containment test pressure 
    for containment leakage testing. Such testing is only performed with 
    the affected unit in the shutdown condition. Therefore, the proposed 
    change in Pa does not involve a significant increase in 
    the probability of an accident previously evaluated.
        All accidents in the Updated Final Safety Analysis Report 
    (UFSAR) were evaluated to determine the effect of an increase in 
    primary volume on accident consequences. The events identified that 
    may be impacted by an increase in primary volume are the Waste Gas 
    System Leak or Failure and LBLOCA. For the Waste Gas System Leak or 
    Failure, the activity of the decay tank is controlled to Technical 
    Specification limits which are unaffected by RCS volume. Therefore, 
    an increase in RCS volume would not increase the offsite dose.
        The offsite dose calculation for the LBLOCA is unaffected by the 
    proposed change. The license basis offsite dose calculation is in 
    accordance with NRC Reg Guide 1.4 ``Assumptions Used for Evaluating 
    The Potential Radiological Consequences of a Loss of Coolant 
    Accident for Pressurized Water Reactors.'' This Regulatory Guide 
    states, in part, ''...a number of appropriately conservation 
    assumptions, based on engineering judgment and on applicable 
    experimental results from safety research programs conducted by the 
    AEC.'' These conservatisms include (but are not limited to) the 
    following assumptions:
         Twenty five percent of the equilibrium radioactive full 
    power inventory is immediately available for leakage from the 
    primary containment.
         100% of the equilibrium full power radioactive noble 
    gas inventory is immediately available for leakage from the primary 
    containment.
         The primary containment should be assumed to leak at 
    the (maximum) leak rate specified in the technical specifications 
    for the first 24 hours and at 50% of this value for the remaining 29 
    days of the accident duration.
        The design basis leakage corresponding to a peak containment 
    pressure of 50 psig utilized in the design basis accident analysis 
    is 0.10% per day of the containment free air mass. Therefore, the 
    offsite dose calculation was performed with a leakage of .1% per day 
    for day one and .05% per day for days two through 30. Isotopic 
    inventories are unaffected by the increase in reactor coolant 
    volume. Thus, the offsite dose is unaffected by the increase in the 
    peak containment pressure. Therefore, this proposed change to 
    Pa does not involve a significant increase in the 
    consequences of an accident previously evaluated.
        The editorial changes proposed are for clarity and consistency 
    within the Technical Specifications and do not affect either the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change in RCS volume is a change in a plant 
    parameter within the ``Design Features'' section of the Technical 
    Specifications. Increasing the RCS volume does not create any new or 
    different failure modes. The existing RCS design requirements 
    continue to be met.
        The revised value of Pa continues to be less than the 
    design basis pressure for the containment building structure. The 
    change represents only a revision to the test pressure for 
    containment leakage testing. Such testing is only performed with the 
    affected unit in the shutdown condition. Therefore, no new or 
    different failure modes are being introduced by modification of the 
    testing parameters.
        The editorial changes proposed are for clarity and consistency 
    within the Technical Specifications and do not result in any 
    physical changes to the facility or how it is operated. No new or 
    different failure modes are being introduced by these changes.
        Therefore, these proposed changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Changing the RCS volume in the Technical Specifications does not 
    reduce the margin of safety. RCS volume is a design feature. The 
    change in RCS volume does not involve a change to any setpoint or 
    design requirements. An evaluation of all UFSAR accidents was 
    performed to determine the effect of an increase in RCS volume. This 
    evaluation is summarized as follows:
        An evaluation of the Chemical and Volume Control System 
    Malfunction was performed to determine the effect of the increased 
    RCS volume due to the RSGs. The larger RCS volume of the RSGs 
    reduces the reactivity insertion for a given dilution flow rate. 
    Therefore, the UFSAR analyses remain bounding for Byron Unit 1 and 
    Braidwood Unit 1 with the RSGs and there is no reduction in the 
    margin of safety.
        An evaluation of the Inadvertent Actuation of the Emergency Core 
    Cooling System During Power Operation Event was performed to 
    determine the effect of the increased RCS volume due to the RSGs. 
    For this event, the injection of borated water causes a negative 
    reactivity insertion, which increases DNBR. For a given Refueling 
    Water Storage Tank (RWST) boron concentration, the larger RCS volume 
    will cause a reduction in the negativity insertion rate as compared 
    to the current UFSAR analysis. However, negative reactivity would 
    still be inserted, no fuel pins would experience DNB, and there is 
    no reduction in the margin of safety.
        An evaluation of the Small Break LOCA was performed to determine 
    the effect of increased RCS volume. The additional RCS volume will 
    cause a delay in the loop seal clearing which in turn delays the 
    core uncovery as compared with the UFSAR analysis. A delay in core 
    uncovery reduces the amount of core heatup which results in a lower 
    peak clad temperature (PCT) because the core decay heat would be 
    less than in the UFSAR analysis. The benefit is considered small, 
    but there is still a benefit. Therefore, the increased RCS volume 
    does not result in a reduction in the margin of safety.
        An evaluation of the Large Break LOCA was performed to determine 
    the effect of increased RCS volume. For a LBLOCA, the increased RCS 
    volume causes the blowdown phase of the event to be longer. 
    Increased blowdown phase, alone, could potentially result in a 
    higher PCT. However, the RSGs also have less resistance to flow due 
    to increased primary side steam generator flow area, which results 
    in a higher blowdown flow compared to the OSGs. The increased 
    blowdown flow more than compensates for the longer blowdown phase 
    associated with the increased RCS volume. The net effect is a 
    decrease in PCT for the RSG compared to the OSG. Therefore, there is 
    no reduction in the margin of safety.
        An evaluation of the Gas Waste System Leak or Failure was 
    performed to determine the effect of the increased RCS volume. 
    Because the activity of the decay tank is controlled within 
    Technical Specification limits, an increase in RCS volume would not 
    change the results of the event. Therefore, there is no reduction in 
    the margin of safety.
        An evaluation was performed to determine the effect of the 
    increased RCS volume on the peak containment pressure following a 
    LBLOCA. The increased RCS volume caused the peak containment 
    pressure to increase to 47.8 psig. This is still below the 
    containment design pressure of 50.0 psig. Therefore, there is no 
    reduction in the margin of safety.
        This proposed change involves testing requirements designed to 
    demonstrate adequate leakage rates are maintained. If adequate 
    leakage rates are maintained as outlined in the Technical 
    Specifications, there will be no reduction in the margin of safety. 
    In the event of degradation of a containment seal that results in 
    unacceptable leakage, plant shutdown will occur as required by 
    Technical Specifications and administrative requirements in 
    accordance with approved plant procedures. Therefore, this proposed 
    change does not involve a significant reduction in a margin of 
    safety.
        The editorial changes proposed are for clarity and consistency 
    within the Technical Specifications and do not result in any 
    physical changes to the facility or how it is
    
    [[Page 19828]]
    
    operated. Therefore, the changes have no effect on the margin of 
    safety.
        Thus, this amendment request does not result in any decrease in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of amendment request: March 27, 1997
        Description of amendment request: The proposed amendment would 
    alter the company name in the Facility Operating License DPR-20 and 
    Technical Specifications for the Palisades Plant. Specifically, the 
    proposed amendment would revise the name from ``Consumers Power 
    Company'' to ``Consumers Energy Company.''
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Since the proposed changes do not alter the technical content of 
    any Facility Operating License or Technical Specifications 
    requirements, they do not alter any feature of plant equipment, 
    settings, operation, or configuration.
        Therefore, they cannot involve a significant increase in the 
    probability of an accident previously evaluated.
        The proposed changes alter the company name in the Facility 
    Operating License and Technical Specifications to reflect the change 
    from ``Consumers Power Company'' to ``Consumers Energy Company''. 
    The proposed change will not affect any obligations. The company 
    will continue to own all of the same assets, will continue to serve 
    the same customers, and will continue to honor all existing 
    obligations and commitments. The proposed changes will not alter 
    plant operation or configuration, or its ability to respond to 
    accidents.
        Therefore, they will not involve a significant increase in the 
    consequences of any accident previously evaluated.
        B. Do the proposed changes create the possibility of a new or 
    different kind of accident from any previously evaluated?
        Since the proposed changes do not alter the technical content of 
    any Facility Operating License or Technical Specifications 
    requirements, they do not alter any feature of plant equipment, 
    settings, operation or configuration.
        Therefore, they cannot create the possibility of a new or 
    different kind of accident from any previously evaluated.
        C. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        Since the proposed changes do not alter the technical content of 
    any Facility Operating License or Technical Specifications 
    requirements, they do not alter any feature of plant equipment, 
    settings, operation, or configuration.
        Therefore, they cannot involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201
        NRC Project Director: John N. Hannon
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of amendment request: March 31, 1997 (TSC 96-10)
        Description of amendment request: The proposed amendments would 
    modify and clarify the High Pressure Injection (HPI) System operability 
    requirements in Specification 3.3.1, impose additional HPI system 
    operability requirements for operation above 75 percent power, 
    incorporate the new Standard Technical Specifications format for the 
    HPI system, revise Specification 3.3.2 to clarify that the Reactor 
    Building Emergency Sump isolation valves are remote-manually operated 
    valves, and add new specifications and a surveillance test to address 
    operability requirements of the atmospheric dump valves. In addition, 
    corresponding Bases changes would be incorporated.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated:
        No. None of the proposed changes has any impact upon the 
    probability of any accident which has been evaluated in the UFSAR 
    [Updated Final Safety Analysis Report]. The only potential change in 
    operating configuration is allowing operation with the HPI [High 
    Pressure Injection] System pump discharge header cross-
        connected. This operating mode does not affect the probability 
    of a LOCA [Loss-of-Coolant Accident] or of any other accident 
    evaluated in the UFSAR.
        None of these changes have any impact upon the ability of the 
    HPI System to add soluble poison to the Reactor Coolant System, as 
    addressed by Specification 3.2. The remaining potential impact is 
    upon the ability to mitigate the consequences of a small break LOCA, 
    which is addressed below. The small break LOCA is the limiting 
    design basis accident with respect to HPI System operability 
    requirements.
        The proposed changes to Specification 3.3.1 provide appropriate 
    actions to address any degradation in the operability of the HPI 
    System. The operability requirements for the HPI System are 
    supported by a spectrum of small break LOCA analyses based on the 
    approved Evaluation Model described in FTI [Framatome Technologies, 
    Incorporated] topical report BAW-10192P. These small break LOCA 
    analyses demonstrate that the acceptance criteria of 10CFR 50.46 are 
    not violated.
        Two trains of HPI are required to mitigate a small break LOCA 
    above 75% FP [full power]. Operability requirements in the proposed 
    Technical Specifications assure that the HPI System can withstand 
    the worst single failure and still result in two HPI pumps injecting 
    through two trains. The full power small break LOCA analyses 
    supporting this proposed license amendment have been performed in 
    accordance with the approved Evaluation Model described in FTI 
    topical report BAW-10192P. The proposed Technical Specifications 
    limit operation above 75% FP with a degraded HPI System to 72 hours 
    before a power reduction to less than 75% FP (or a reactor shutdown) 
    must be initiated. The required actions depend on the HPI System 
    components that are inoperable. The 72 hour completion time is 
    consistent with the time requirements for HPI specified in NUREG-
    1430.
        When at or below 75% FP, one HPI train provides sufficient flow 
    to mitigate a small break LOCA. The 75% power level is justified by 
    analyses using the Evaluation Model described in FTI topical report 
    BAW-10192P, considering the worst case break location and size 
    described in LER [Licensee Event Report] 269/90-15 and Attachment 3 
    to this submittal. The proposed Technical Specifications require two 
    HPI trains to be operable at or below 75% FP. These requirements 
    ensure that, following the worst single failure, one train of HPI 
    would remain
    
    [[Page 19829]]
    
    available to mitigate a small break LOCA. Operation with less than 
    two HPI trains operable is restricted to 72 hours before shutdown 
    requirements are imposed. This completion time is consistent with 
    the time requirements specified for an HPI System in NUREG-1430.
        The additional HPI system restriction that requires the HPI pump 
    discharge header to be cross-connected when all three HPI pumps are 
    operable does not increase the consequences of a small break LOCA. 
    If a single failure prevents one HPI train from actuating, this 
    lineup results in at least two HPI pumps initially injecting through 
    the automatically actuating train. This increases the amount of 
    cooling flow initially delivered to the core as compared to the 
    current system configuration.
        The impact of this alignment has been evaluated, considering the 
    potential single active failures, including the failure of any 
    powered component to operate and any single failure of electrical 
    equipment.
        It has been determined that, when each of the three HPI pumps is 
    either running or is capable of automatic actuation upon an 
    Engineered Safeguards signal, cross-connection of the HPI pump 
    discharge header does not introduce susceptibility to any single 
    failure. Therefore, the potential consequences of a small break LOCA 
    are not increased. If fewer than three HPI pumps are either running 
    or are capable of automatic actuation, and the HPI pump discharge 
    header were cross-connected, a single failure of one pump could 
    cause a single pump to be aligned to both HPI trains. In this 
    condition, the single pump could experience runout conditions prior 
    to corrective operator action. However, proposed Specification 3.3.1 
    requires the discharge header to be isolated between the two 
    remaining operable HPI pumps. The proposed BASES provide guidelines 
    to ensure that the requirements for redundancy are properly 
    implemented. Therefore, the proposed specifications ensure that the 
    consequences of a small break LOCA are not increased by allowing the 
    HPI pump discharge header to be cross-connected.
        In addition, proposed Specification 3.4.7 requires new 
    operability requirements for the main steam atmospheric dump valves. 
    These operability requirements do not impact the probability or 
    consequences of any accident. The proposed specification for the 
    atmospheric dump valves provides additional assurance that these 
    valves will be operable in the event of a small break LOCA.
        In summary, the proposed Technical Specifications provide 
    adequate controls to assure that operability of the HPI System is 
    maintained in a manner consistent with the requirements of the 
    design basis accidents. Therefore, it is concluded that this 
    amendment request will not significantly increase the probability or 
    consequences of an accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any kind of accident previously evaluated:
        No. Of the proposed substantive changes, only cross-connection 
    of the HPI pump discharge header represents any change to the way in 
    which the facility is normally operated. Operation with the 
    discharge header cross-connected is not a new configuration, as it 
    has always been used for HPI pump testing both at power and during 
    shutdown conditions. Potential failure modes have already been 
    considered as described earlier. No new initiating events or 
    potentially unanalyzed conditions have been created. Therefore, this 
    proposed amendment will not create the possibility of any new or 
    different kind of accident.
        (3) Involve a significant reduction in a margin of safety.
        No. The HPI restrictions associated with the proposed Technical 
    Specifications are supported by analyses which demonstrate that the 
    acceptance criteria of 10 CFR 50.46 are not violated for any small 
    break LOCA. These analyses were performed in accordance with the 
    Evaluation Model described in FTI topical report BAW-10192P. 
    Therefore, it is concluded that the proposed amendment request will 
    not result in a significant decrease in the margin of safety.
        Duke has concluded, based on the above, that there are no 
    significant hazards considerations involved in this amendment 
    request.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: March 10, 1997
        Description of amendment request: The proposed amendment would 
    modify Technical Specification 3.4.5, ``Steam Generators,'' and 
    associated Bases to allow repair of steam generator tubes by 
    installation of sleeves with the tungsten inert gas (TIG) welded sleeve 
    developed by ABB Combustion Engineering. In addition, the proposed 
    amendment would delete the option for using the kinetic sleeving 
    methodology previously approved for use at Beaver Valley, but is not 
    currently recommended by Framatome Technologies, Inc.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed amendment allows the ABB Combustion Engineering 
    (ABB/CE) tungsten inert gas (TIG) welded tubesheet sleeves and tube 
    support plate sleeves to be used as an alternate steam generator 
    tube repair method. The sleeve configuration was designed and 
    analyzed in accordance with the criteria of Regulatory Guide (RG) 
    1.121 and Section III of the ASME [American Society of Mechanical 
    Engineers] Code. Fatigue and stress analyses of the sleeved tube 
    assemblies produce acceptable results for both types of sleeves as 
    documented in ABB/CE Topical Report CEN-629-P, Revision 02 and CEN-
    629-P Addendum 1. Mechanical testing has shown that the structural 
    strength of the sleeves under normal, faulted, and upset conditions 
    is within the acceptable limits specified in RG 1.121. Leakage rate 
    testing for the tube sleeves has demonstrated that primary to 
    secondary leakage is not expected during any plant condition. The 
    consequences of leakage through the sleeved region of the tube is 
    fully bounded by the existing steam generator tube rupture (SGTR) 
    analysis included in the Updated Final Safety Analysis Report 
    (UFSAR).
        The sleeves are designed to allow inservice inspection of the 
    pressure retaining portions of the sleeve and parent tube. Inservice 
    inspection is performed on all sleeves following installation to 
    ensure that each sleeve has been properly installed and is 
    structurally sound. Periodic inspections are performed in subsequent 
    refueling outages to monitor sleeve degradation on a sample basis. 
    The eddy current technique used for inspection will be capable of 
    detecting both axial and circumferential flaws. Specific guidance 
    for steam generator sleeve inspection is provided in the current 
    technical specification surveillance requirements. Tubes that 
    contain defects in a sleeve, which exceed the repair limit, will be 
    removed from service. This ensures that sleeve and tube structural 
    integrity is maintained.
        The proposed TS change to support the installation of TIG welded 
    sleeves does not adversely impact any previously evaluated design 
    basis accident. The effect of sleeve installation on the performance 
    of the SG [steam generator] was analyzed for heat transfer, flow 
    restriction, and steam generation capacity. The sleeves reduce the 
    risk of primary to secondary leakage in the SG. The installation of 
    ABB/CE sleeves results in a hydraulic flow restriction that is 
    dependent on the number and types of sleeves installed. The 
    reduction in primary system flow rate is a small percentage of the 
    flow rate reduction seen from plugging one tube and is a preferable 
    alternative when considering core margins based on minimum reactor 
    coolant system flow rates. The sleeving installation will result in 
    a resistance to primary coolant flow through the tube for other 
    evaluated accidents. The results of the analyses and testing, as 
    well as industry operating experience, demonstrate that the sleeve 
    assembly is an acceptable
    
    [[Page 19830]]
    
    means of maintaining tube integrity. In summary, installation of 
    sleeves does not substantially affect the primary system flow rate 
    or the heat transfer capability of the steam generators.
        Installation of the sleeves can be used to repair degraded tubes 
    by returning the condition of the tubes to their original design 
    basis condition for tube integrity and leak tightness during all 
    plant conditions. The tube bundle overall structural and leakage 
    integrity will be increased with the installation of the sleeves 
    reducing the risk of primary to secondary leakage in the SG while 
    maintaining acceptable reactor coolant system flow rates. Therefore, 
    sleeving will not increase the probability of occurrence of an 
    accident previously evaluated.
        Removal of the kinetically welded sleeve process as an approved 
    SG tube repair methodology will have no effect on plant operations. 
    There are currently no kinetically welded sleeves installed in the 
    steam generators. Had there been, plant operations would have still 
    been bounded by the existing SGTR analysis in the UFSAR.
        Therefore, these proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The implementation of the proposed sleeving process will not 
    introduce significant or adverse changes to the plant design basis. 
    Stress and fatigue analyses of the repair has shown the ASME Code 
    Section III and RG 1.121 allowable values are met. Implementation of 
    TIG welded sleeving maintains overall tube bundle structural and 
    leakage integrity at a level consistent with that of the originally 
    supplied tubing. Leak and mechanical testing of the sleeves support 
    the conclusions that the sleeve retains both structural and leakage 
    integrity during all conditions. Repair of a tube with a sleeve does 
    not provide a mechanism that would result in an accident outside of 
    the area affected by the sleeve.
        Any hypothetical accident as a result of potential tube or 
    sleeve degradation in the repaired portion of the tube is bounded by 
    the existing SGTR analysis. The SGTR analysis accounts for the 
    installation of sleeves and the impact on current plugging level 
    analyses. The sleeve design does not affect any other component or 
    location of the tube outside of the immediate area repaired.
        The current primary to secondary leakage limit ensures that SG 
    tube integrity is maintained in the event of an MSLB [main steam 
    line break] or LOCA [loss-of-coolant accident]. The limit will 
    provide for leakage detection and a plant shutdown in the event of 
    the occurrence of an unexpected single crack resulting in excessive 
    tube leakage. The leakage limit also provides for early detection 
    and a plant shutdown prior to a postulated crack reaching critical 
    crack lengths for MSLB conditions.
        Inservice inspections are performed following sleeve 
    installation to ensure proper weld fusion has occurred to maintain 
    structural integrity. The post installation inspection also serves 
    as baseline data to be used for comparison during future 
    inspections. Periodic eddy current inspections monitor the pressure 
    retaining portions of the sleeve and parent tube for degradation. 
    Eddy current techniques will be employed that are sensitive to axial 
    and circumferential degradation.
        Increasing the sample size of tubes repaired using either 
    sleeving process during each scheduled inservice inspection will 
    increase the monitoring of these tubes for any further degradation. 
    The improved monitoring and evaluation of the tube and the sleeves 
    assures tube structural integrity is maintained or the tube is 
    removed from service.
        Corrosion testing of typical sleeve-tube configurations was 
    performed to evaluate local stresses, sleeve life, and resistance to 
    primary and secondary side corrosion. The tests were performed on 
    stress relieved and as-welded (non-stress relieved) sleeve-tube 
    joints. Using the corrosion test data in conjunction with finite 
    element analyses of the local stress, the stress relieved joint life 
    was determined to be in excess of 40 years. The ABB/CE TIG welded 
    sleeve operating experience in the industry has shown no sleeve 
    failures due to service induced degradation in sleeves that were 
    installed with acceptable inspection results. This experience 
    includes the stress relieved and as-welded sleeve configurations. 
    All sleeves will be stress relieved as specified in the topical 
    report.
        Removal of the kinetically welded sleeve process as an approved 
    SG tube repair methodology and not completing the additional 
    corrosion testing necessary to establish the design life for the 
    kinetically welded sleeve in the presence of a crevice will not 
    create the possibility of a new or different type of accident from 
    any accident previously evaluated.
        Repair of an SG tube with a kinetically welded sleeve would not 
    have provided a mechanism that resulted in an accident outside of 
    the area affected by the sleeve. Any hypothetical accident as a 
    result of potential tube or sleeve degradation in the repaired 
    portion of the tube would have been bounded by the existing SGTR 
    analysis. The SGTR analysis accounts for the installation of sleeves 
    and the impact on current plugging level analyses. The sleeve design 
    does not affect any other component or location of the tube outside 
    of the immediate area repaired. Furthermore, there are currently no 
    kinetically welded sleeves installed in either plant.
        Therefore, the proposed changes do not create the possibility of 
    a new or different type of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The TIG welded sleeving repair of degraded steam generator tubes 
    has been shown by analysis to restore the integrity of the tube 
    bundle to its original design basis condition. The safety factors 
    used in the design of the sleeves for the repair of degraded tubes 
    are consistent with the safety factors in the ASME Boiler and 
    Pressure Vessel Code Section III used in steam generator design. The 
    design of the ABB/CE SG sleeves has been verified by testing to 
    preclude leakage during normal and postulated accident conditions.
        The portion of the installed sleeve assembly which represents 
    the reactor coolant pressure boundary can be monitored for the 
    initiation and progression of sleeve/tube wall degradation, thus 
    satisfying the requirement of RG 1.83. The portion of the SG tube 
    bridged by the sleeve joints is effectively removed from the 
    pressure boundary, and the sleeve then forms the new pressure 
    boundary. The sleeve enhances the safety of the plant by 
    reestablishing the protective boundaries of the steam generator. 
    Keeping the tube in service with the use of a sleeve instead of 
    plugging the tube and removing it from service increases the heat 
    transfer efficiency of the steam generator. During each scheduled 
    inservice inspection, each sleeve inspected and found to have 
    unacceptable degradation shall be removed from service.
        The effect on the design transients and the accident analyses 
    have been revised based on the installation of sleeves equal to the 
    tube plugging level coincident with the minimum reactor coolant flow 
    rate. Evaluation of the installation of sleeves was based on the 
    determination that LOCA evaluations for the licensed minimum reactor 
    coolant flow bound the combined effect of tube plugging and sleeving 
    up to an equivalent of the actual plugging limit. Sleeving results 
    in a fractional amount of the plugging limitation of one tube and is 
    a preferable alternative when considering core margins based on 
    minimum reactor coolant system flow rates. The sleeving installation 
    will result in a resistance to primary coolant flow through the 
    tube. The primary coolant flow through the ruptured tube is reduced 
    by the influence of the installed sleeve; therefore, the 
    consequences to the public due to an SGTR event have not increased.
        As SG sleeve removes an indication of a possible leak source 
    from the reactor coolant system (RCS) pressure boundary, eliminating 
    the potential of a primary-to-secondary leak. The structural 
    integrity of the tube is maintained by the sleeve and sleeve-to-tube 
    joint.
        Installation of either tube sheet or tube support plate sleeves 
    will increase the protective boundaries of the steam generators and 
    will not reduce the margin of safety.
        Removal of the kinetically welded sleeve process as an approved 
    SG tube repair methodology will not result in a reduction in the 
    margin of safety. There are currently no kinetically welded sleeves 
    installed in either plant. SG tube integrity will be maintained by 
    applying an alternate NRC approved repair methodology or removing 
    the SG tube from service by plugging.
        Therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
    [[Page 19831]]
    
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: March 10, 1997
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications 3.4.5, ``Steam Generators,'' and 
    associated Bases to allow repair of steam generator tubes by 
    installation of sleeves with the Electrosleeving process developed by 
    Framatome Technologies, Inc. (FTI).
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The Electrosleeve configuration has been designed and analyzed 
    in accordance with the requirements of the ASME [American Society of 
    Mechanical Engineers] Code. The applied stresses and fatigue usage 
    for the Electrosleeve are bounded by the limits established in the 
    ASME Code. Minimum material property values are used for the 
    structural and plugging limit analysis. Mechanical testing has shown 
    that the structural strength of nickel Electrosleeves under normal, 
    upset, and faulted conditions provides margin to the acceptance 
    limits. These acceptance limits bound the most limiting (3 times 
    normal operating pressure differential) burst margin recommended by 
    Regulatory Guide 1.121. Leakage testing has shown that the 
    Electrosleeve is essentially leaktight during all plant conditions.
        The Electrosleeve nominal wall thickness depth-based plugging 
    limit is determined using the guidance of Regulatory Guide 1.121 and 
    the pressure stress equation of Section III of the ASME Code. The 
    limiting requirement of Regulatory Guide 1.121 for the 
    Electrosleeve, which applies to part through wall degradation, is 
    the minimum acceptable wall thickness to maintain a safety factor of 
    three against tube failure under normal operating conditions. A 
    bounding set of design and transient loading input conditions was 
    used for the minimum wall thickness evaluation in the generic 
    evaluation. Evaluation of the minimum acceptable wall thickness for 
    normal, upset and postulated accident condition loading per the ASME 
    Code indicates these conditions are bounded by the design minimum 
    wall thickness.
        Bounding tube wall degradation growth rate per cycle and 
    nondestructive examination uncertainty has been assumed for 
    determining the Electrosleeve technical specification plugging 
    limit. Electrosleeve wall degradation extent determined by 
    nondestructive examination, which would require plugging 
    Electrosleeved tubes, is developed using the guidance of Regulatory 
    Guide 1.121 and is defined in FTI Topical Report BAW-10219P, 
    Revision 1, to be 20% throughwall of the nominal sleeve wall 
    thickness.
        The effect of Electrosleeving and plugging will remain below the 
    plugging limit assumed in the UFSAR [Updated Final Safety Analysis 
    Report]. The proposed change will not increase the consequences of 
    these accidents.
        The results of the analyses and testing demonstrate that the 
    Electrosleeve is an acceptable means of maintaining tube integrity. 
    Further, per Regulatory Guide 1.83 recommendations, the 
    Electrosleeved tube can be monitored through periodic inspections 
    with present NDE [nondestructive examination] techniques. These 
    measures demonstrate that installation of Electrosleeves spanning 
    degraded areas of the tube will restore the tube to a condition 
    consistent with its original design basis.
        Since the main steamline break post-accident primary-to-
    secondary leakage is not increased by the presence of 
    Electrosleeves, the consequences of an accident previously evaluated 
    in the UFSAR are not increased. Conformance of the Electrosleeve 
    design with the applicable sections of the ASME Code and results of 
    the leakage and mechanical tests support the conclusion that 
    installation of Electrosleeves does not increase the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Electrosleeving will not adversely affect any plant component. 
    Stress and fatigue analysis of the repair has shown that the ASME 
    Code and Regulatory Guide 1.121 criteria are not exceeded. 
    Implementation of Electrosleeving maintains overall tube bundle 
    structural and leakage integrity at a level consistent with that of 
    the original tubing during all plant conditions. Leak and mechanical 
    testing of Electrosleeves support the conclusions of the 
    calculations that each Electrosleeve retains both structural and 
    leakage integrity during all conditions. Electrosleeving of tubes 
    does not provide a mechanism resulting in an accident outside of the 
    area affected by the Electrosleeves. Any accident resulting from 
    potential tube or Electrosleeve degradation in the repaired portion 
    of the tube is bounded by the existing tube rupture accident 
    analysis.
        Implementation of Electrosleeving will reduce the potential for 
    primary-to-secondary leakage while not significantly impacting 
    available primary coolant flow area in the event of a LOCA. By 
    effectively isolating degraded areas of the tube through repair, the 
    potential for steamline break leakage is reduced. These degraded 
    intersections now are returned to a condition consistent with the 
    Design Basis. While the installation of an Electrosleeve reduces 
    primary coolant flow, the reduction is far below that caused by 
    plugging. Greater primary coolant flow area is maintained through 
    Electrosleeving versus plugging. Therefore, the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    is not created.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The Electrosleeve repair of degraded steam generator tubes has 
    been shown by analysis to restore the integrity of the tube bundle 
    consistent with its original design basis condition. The tube/
    Electrosleeve operational and faulted condition stresses are bounded 
    by the ASME Code requirements and the Electrosleeved tubes are 
    leaktight. The safety factors used in the design of Electrosleeves 
    for the repair of degraded tubes are consistent with the safety 
    factors in the ASME Code used in steam generator design. The 
    portions of the installed Electrosleeve assembly which represent the 
    reactor coolant pressure boundary can be monitored for the 
    initiation and progression of Electrosleeve/tube wall degradation, 
    thus satisfying the requirements of Regulatory Guide 1.83. The 
    portion of the tube bridged by the Electrosleeve is effectively 
    removed from the pressure boundary, and the Electrosleeve then forms 
    the new pressure boundary. The areas of the Electrosleeved tube 
    assembly which require inspection are defined in Framatome 
    Technologies Inc. Topical Report BAW-10219P, Revision 1.
        In addition, since the installed Electrosleeve represents a 
    portion of the pressure boundary, a baseline inspection of these 
    areas is required prior to operation with Electrosleeves installed. 
    The effect of sleeving on the design transients and accident 
    analyses has been reviewed based on the installation of 
    Electrosleeves up to the level of steam generator tube plugging 
    coincident with the minimum reactor coolant flow rate and UFSAR and 
    has been found acceptable.
        It is concluded that the proposed license amendment request does 
    not result in a significant reduction in the margin of safety as 
    defined in the UFSAR or technical specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London, 
    Connecticut
    
        Date of amendment request: March 27, 1997
    
    [[Page 19832]]
    
        Description of amendment request: The proposed changes to the 
    Technical Specifications (TSs) would modify the limiting condition for 
    operation (LCO) and surveillance requirements (SR) for the ultimate 
    heat sink. The ultimate heat sink for Millstone Unit No. 2 is the Long 
    Island Sound that transfers heat from safety-related systems during 
    normal and accident conditions. Specifically, TS LCO 3.7.11 would be 
    changed to indicate that the ultimate heat sink is operable at a water 
    temperature of less than or equal to 75  deg.F instead of an average 
    value. TS SRs 4.7.11.a and .b would also delete the use of average when 
    verifying the water temperature and delete the reference to a specific 
    monitoring location, the Unit No. 2 intake structure. These proposed 
    changes do not change the ultimate heat sink temperature limit, which 
    remains at a maximum of 75  deg.F.
        The TS Bases 3/4.7.11 would also be modified to reflect the above 
    changes and to identify the various locations that the ultimate heat 
    sink temperature can be measured.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve an SHC [significant hazards 
    consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes remove the reference to a monitoring 
    location where the temperature of the ultimate heat sink is measured 
    and eliminate the use of an average ultimate heat sink temperature. 
    The instruments used provide information to the operators which will 
    permit them to ensure that the plant is operated within the design 
    basis of the plant. The subject instruments will provide an accurate 
    representation of the ultimate heat sink temperature. This role is 
    passive; thus, these instruments cannot initiate or mitigate any 
    accident.
        The locations used to monitor the ultimate heat sink temperature 
    will be maintained in the Bases. This is a licensee controlled 
    document which is maintained under the requirements of 10CFR50.59. 
    The details being removed from the Technical Specifications are not 
    assumed to be an initiator of any analyzed event. Since any changes 
    to the relocated details will be evaluated per 10CFR50.59, any 
    possible increase in the probability or consequences of an accident 
    previously evaluated will be addressed.
        The proposed changes do not revise the ultimate heat sink 
    temperature limit of 75  deg.F. The current analysis is based on the 
    ultimate heat sink temperature limit of 75  deg.F. Therefore, there 
    is no effect on the consequences of any accident previously 
    evaluated.
        Thus, the license amendment request does not impact the 
    probability of an accident previously evaluated nor does it involve 
    a significant increase in the consequences of an accident previously 
    evaluated.
        2. Created the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed changes remove the reference to a monitoring 
    location where the temperature of the ultimate heat sink is measured 
    and eliminate the use of an average ultimate heat sink temperature. 
    The instruments used provide information to the operators which will 
    permit them to ensure that the plant is operated within the design 
    basis of the plant. The subject instruments will provide an accurate 
    representation of the ultimate heat sink temperature. This role is 
    passive, thus, these instruments cannot initiate or mitigate any 
    accident.
        The proposed changes will not alter the plant configuration (no 
    new or different type of equipment will be installed) or require any 
    new or unusual operator actions. They do not alter the way any 
    structure, system, or component functions and do not alter the 
    manner in which the plant is operated. The proposed changes do not 
    introduce any new failure modes. They will not alter assumptions 
    made in the safety analysis and licensing basis.
        The locations used to monitor the ultimate heat sink temperature 
    will be maintained in the Bases. This is a licensee controlled 
    document which is maintained under the requirements of 10CFR50.59. 
    Thus, adequate control of information will be ensured.
        Therefore, the changes will not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes remove the reference to a monitoring 
    location where the temperature of the ultimate heat sink is measured 
    and eliminate the use of an average ultimate heat sink temperature. 
    They do not change the ultimate heat sink temperature limit of 75 
    deg.F, which is assumed by the current analysis. Therefore, there is 
    no effect on the consequences of any accident previously evaluated 
    and no significant impact on offsite doses associated with 
    previously evaluated accidents. Thus, there is no significant 
    reduction in the margin of safety for the design basis accident 
    analysis. The license amendment request does not result in a 
    reduction of the margin of safety as defined in the Bases for 
    Technical Specification 3.7.11. The instruments used provide 
    information to the operators which will permit them to ensure that 
    the plant is operated within the design basis of the plant. The 
    subject instruments will provide an accurate representation of the 
    ultimate heat sink temperature. The proposed changes do not alter 
    the way any structure, system, or component functions and do not 
    alter the manner in which the plant is operated. They do not have 
    any impact on the protective boundaries (e.g., fuel matrix and 
    cladding, reactor coolant system pressure boundary, and primary and 
    secondary containment), or on the safety limits for these 
    boundaries.
        The locations used to monitor the ultimate heat sink temperature 
    will be maintained in the Bases. The Bases are a licensee controlled 
    document which is maintained under the requirements of 10CFR50.59. 
    Since any future changes to this license controlled document will be 
    evaluated per the requirements of 10CFR50.59, any possible reduction 
    (significant or insignificant) in a margin of safety will be 
    addressed.
        Thus, the license amendment request does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270NRC Deputy Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: March 31, 1997
        Description of amendment request: The proposed amendment would 
    modify Technical Specification Surveillance Requirement 4.7.1.2.1.b 
    which requires the testing of the auxiliary feedwater motor-driven and 
    turbine-driven pumps on recirculation flow at least once per 92 days. 
    The proposed amendment would also makes changes to the appropriate 
    Bases section.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed changes in accordance with 10CFR 
    50.92 and has concluded that the changes do not involve a 
    significant hazards consideration (SHC). The bases for this 
    conclusion is that the three criteria of 10CFR 50.92(c) are not 
    satisfied. The proposed changes do not involve [an] SHC because the 
    changes would not:
    
    [[Page 19833]]
    
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed changes to Technical Specification Surveillance 
    4.7.1.2.1.b to increase the required test parameter for the motor 
    driven pumps from 1460 psid to 1468 psid and replacing the current 
    parameters for the motor driven and turbine driven pumps from 
    differential pressure measured in psid [pounds per square inch 
    differential] to total head measured in feet are consistent with 
    equipment design criteria and does not significantly increase the 
    probability of an accident previously evaluated.
        The proposed changes to increase the required test parameter for 
    the motor driven pumps from 1460 psid to 1468 psid and replacing the 
    current parameters for the motor driven and turbine driven pumps 
    from differential pressure measured in psid to total head measured 
    in feet provides the necessary assurance that the pumps will 
    function as required in accident analyses and does not significantly 
    increase the consequence of an accident previously evaluated.
        The moving of the reference to Specification 4.0.5 in order to 
    clarify that it applies to the testing of the motor driven and 
    turbine driven pumps and the modifications to the bases section are 
    administrative and do not involve a significant increase in the 
    probability or consequence of an accident previously evaluated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to Technical Specification Surveillance 
    4.7.1.2.1.b to increase the required test parameter for the motor 
    driven pumps from 1460 psid to 1468 psid and replacing the current 
    parameters for the motor driven and turbine driven pumps from 
    differential pressure measured in psid to total head measured in 
    feet does not change the operation of the auxiliary feedwater system 
    or any of its components during normal or accident evaluations.
        The moving of the reference to Specification 4.0.5 in order to 
    clarify that it applies to the testing of the motor driven and 
    turbine driven pumps and the modifications to the bases section are 
    administrative and do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to Technical Specification Surveillance 
    4.7.1.2.1.b to increase the referenced total head of the motor
        driven auxiliary feedwater pumps during surveillance testing 
    provides an acceptable margin between the required surveillance and 
    design pump performance to provide assurance that the pumps will 
    operate consistent with system evaluations and does not involve a 
    significant reduction in a margin of safety.
        The change in the referenced units from differential pressure 
    measured in psid to total head measured in feet for the motor driven 
    auxiliary and turbine driven auxiliary feedwater pumps during 
    surveillance testing is to account for the effect of water density 
    on pump performance during each test and does not involve a 
    significant reduction in a margin of safety.
        The moving of the reference to Specification 4.0.5 in order to 
    clarify that it applies to the testing of the motor driven and 
    turbine driven pumps and the modifications to the bases section are 
    administrative and do not involve a significant reduction in a 
    margin of safety.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed changes do not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270NRC Deputy Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: March 31, 1997
        Description of amendment request: The proposed amendment would 
    separate the required testing of motor-operated valve thermal overload 
    protection into two new surveillances.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed change in accordance with 
    10CFR50.92 and has concluded that the change does not involve a 
    significant hazards consideration (SHC). The bases for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed change does not involve a SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed changes to the surveillance testing of the motor-
    operated valve thermal overload protection are consistent with 
    equipment design criteria and performing surveillance testing does 
    not significantly increase the probability of an accident previously 
    evaluated. The proposed changes to the surveillance testing provides 
    the necessary assurance that the motor operated valve thermal 
    overload protection will function as required and does not involve a 
    significant increase in the consequence of an accident previously 
    evaluated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to the surveillance testing of the motor-
    operated valve thermal overload protection does not change the 
    operation of any system or system component during normal or 
    accident evaluations.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to the surveillance testing of the motor-
    operated valve thermal overload protection are administrative in 
    that the changes to the surveillance only clarify that following 
    maintenance on the motor starter, a channel calibration is required 
    only on that valve. The surveillance continues to require periodic 
    representative sample testing.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed change does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270NRC Deputy Director: Phillip F. McKee
    
    [[Page 19834]]
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: March 4, 1997
        Description of amendment request: The amendments would modify the 
    Emergency Core Cooling System (ECCS) surveillance test acceptance 
    criteria in Technical Specification 3/4.5.2 for the Centrifugal 
    Charging (CH) and the Safety Injection (SI) pumps. The changes to the 
    specified flow values would account for system alignments that effect 
    the suction pressure to the pumps. In the recirculation mode, increased 
    flow occurs when the CH and SI pumps take suction from the discharge of 
    the Residual Heat Removal pumps.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The evaluations performed by Westinghouse determined 
    that, with the proposed changes, the subject pumps remain operable 
    and the safety analyses criteria remain valid.
        Previous conclusions under LCR [License Change Request] 91-03 
    evaluating the consequences of the LOCA [loss-of-coolant-accident] 
    considered in the Salem Units 1 & 2 licensing basis remain 
    unchanged. With respect to the LOCA, the Peak Cladding Temperature 
    (PCT) continues to conform to the 10CFR50.46 guidelines of less than 
    2200*F. Evaluation of LOCA mass and energy releases previously found 
    acceptable remain valid. Decreasing the acceptance window to 
    accommodate the potential of an increase to pump runout flow, 
    assures that the current limits on pump runout flows continue to be 
    met. This change ensures pump integrity is maintained during the 
    accident. The reduction of the flow by throttling valves to 
    compensate for the potential suction boost remains within the 
    current analyses and therefore more conservative values are being 
    proposed. Additionally, the proposed change balances the pump flows 
    more appropriately by differentiating between the hot and cold leg 
    alignments. Flow to the reactor core is unaffected by the very 
    slight reduction in the upper flow limits. Since the design 
    limitations continue to be met and the integrity of the reactor 
    coolant system pressure boundary is not challenged, offsite dose 
    assumptions and calculations remain valid. Further, the ECCS is 
    post-accident mitigation system and probability of an accident is 
    not increased by this proposed change. Lastly, the correction of 
    double use of the word ``the'' in Salem Unit 1 Technical 
    Specification section 4.5.2.h.1.a is of editorial nature.
        Based on the above information, the proposed changes do not 
    increase the risk or consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. No new single failures are initiated. The proposed 
    changes will therefore not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The proposed change addresses suction boost by changing the 
    Technical Specification surveillance acceptance criteria. The 
    typographical correction is of editorial nature.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety. The evaluation of LOCA accident analysis 
    previously performed by Westinghouse continues to be met and 
    verifies that, with the proposed changes to the TS, plant operations 
    will be maintained within the bounds of safe, analyzed conditions as 
    defined in the UFSAR [Updated Final Safety Analysis Report] and that 
    conclusions presented in the UFSAR remain valid. The peak cladding 
    temperatures (PTC) remains unchanged as no effective differences in 
    the operating parameters have occurred. The typographical correction 
    is of editorial nature. The proposed changes will therefore not 
    reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, NJ 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama
    
        Date of amendments request: March 7, 1997
        Description of amendments request: The proposed amendments would 
    allow operability testing for the containment isolation valves listed 
    in Table 3.6-1 of the Technical Specifications during a defueled 
    status. These proposed changes are technically consistent with the 
    requirements of NUREG-1431, Revision 1, ``Westinghouse Standard 
    Technical Specifications,'' issued on April 7, 1995.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.]
        The proposed changes do not significantly increase the 
    probability or consequences of an accident previously evaluated in 
    the FSAR [Final Safety Analysis Report]. The proposed changes have 
    no impact on the probability of an accident. The containment 
    isolation valves will continue to require operability testing. 
    Allowing the testing to be performed when the unit is in a defueled 
    status will have no impact on any accidents previously evaluated. 
    The net effect of these changes is not significant and, as a result, 
    does not involve a significant increase in the consequences of an 
    accident previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated.]
        The proposed changes to the Technical Specifications do not 
    increase the possibility of a new or different kind of accident than 
    any accident already evaluated in the FSAR. No new limiting single 
    failure or accident scenario has been created or identified due to 
    the proposed changes. Safety-related systems will continue to 
    perform as designed. The proposed changes do not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        [3. Involve a significant reduction in a margin of safety.]
        The proposed changes do not involve a significant reduction in 
    the margin of safety. Although, as a result of these proposed 
    changes, the containment isolation valves could be tested for 
    operability while the unit is in a defueled state, there is no 
    impact in the accident analyses. These proposed changes are 
    technically consistent with the requirements of NUREG-1431, Revision 
    1 which has already received the requisite review and approval of 
    the NRC staff. Thus the proposed changes do not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: Herbert N. Berkow
    
    [[Page 19835]]
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: August 22, 1996, as supplemented on 
    March 28, 1997 (TS 96-02)
        Description of amendment request: The proposed changes would revise 
    Section 3.6.5 of the Sequoyah Technical Specifications (TS) and 
    associated Bases to lower the minimum TS ice basket weight of 1,155 
    pounds to 1,071 pounds. This would reduce the overall weight of ice 
    required in the ice condenser from 2,245,320 pounds to 2,082,024 
    pounds. The TVA license amendment request also proposed to extend the 
    chemical analysis surveillance interval for the ice condenser ice bed 
    from 12 months to 18 months based on the provisions of Generic Letter 
    93-05.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of Sequoyah Nuclear Plant (SQN) in accordance with the 
    proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        TVA proposes to modify the SQN Unit 1 and Unit 2 TSs [Technical 
    Specifications] to revise Surveillance Requirement (SR) 4.6.5.1.d to 
    lower SQN's minimum TS basket weight from 1,155 pounds (lbs) to 
    1,071 lbs, thus lowering the overall ice condenser weight from 
    2,245,320 lbs to 2,082,024 lbs.
        The ice condenser system is provided to absorb thermal energy 
    release following a loss-of-coolant accident (LOCA) or high energy 
    line break (HELB) and to limit the peak pressure inside containment. 
    The current containment analysis for SQN is based on a minimum of 
    993 lbs of ice per basket evenly distributed throughout the ice 
    condenser at the end of an 18-month refueling cycle. The revised 
    containment analysis shows that for the predicted sublimation rate 
    of 15 percent for 18 months, an average basket weight of 922 lbs at 
    the end of the 18-month period would ensure containment design 
    pressure is not exceeded.
        Based on TVA's evaluation and the revised containment analysis, 
    TVA considers the reduction of ice weight to be acceptable for 
    satisfying the safety function of the ice condenser for an 18-month 
    ice weighing interval. Therefore, the proposed change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        TVA is also proposing to extend the surveillance interval as it 
    pertains to the ice bed chemical analysis. Based on test results, 
    both at SQN and the industry, the average boron concentration and pH 
    changes are minimal; therefore, this change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        Elimination of the temperature at which the pH of the ice bed is 
    determined is an administrative change. Future testing will be 
    accomplished in accordance with American Society for Testing and 
    Materials Standards recommendations. Therefore, this change cannot 
    increase the probability of an accident and the consequences of an 
    accident will not increase.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        TVA's request to lower the TS limit for ice weight at the start 
    of the surveillance interval will not result in a new or different 
    kind of accident from that previously analyzed in SQN's Final Safety 
    Analysis
        Report. SQN's ice condenser serves to limit the peak pressure 
    inside containment following a LOCA. TVA has evaluated the revised 
    containment pressure analysis for SQN (Enclosure 4, Westinghouse 
    WCAP-12455, Revision 1) and determined that sufficient ice would be 
    present at all times to keep the peak containment pressure below 
    SQN's containment design pressure of 12 pounds per square inch gage 
    (psig). Therefore, this change would not result in a new or 
    different kind of accident from any previously analyzed.
        The proposed reduced testing frequency of the chemical 
    composition of the ice bed does not change the manner in which the 
    plant is operated. Additionally, the ice condenser is a passive 
    system that reacts to an accident, but does not support plant 
    operation on a daily basis. The reduced testing frequency of the ice 
    bed chemical composition does not generate any new accident 
    precursors; therefore, the possibility of a new or different kind of 
    accident from any previously analyzed is not created.
        Elimination of the temperature at which the pH of the ice bed is 
    determined is an administrative change. This change cannot create 
    the possibility of a new or different kind of accident.
        3. Involve a significant reduction in a margin of safety.
        The ice condenser system is provided to absorb thermal energy 
    release following a LOCA and to limit the peak pressure inside 
    containment. The current ice condenser analysis for SQN is based on 
    a minimum of 993 lbs of ice per basket. The revised containment 
    analysis changes the minimum ice weight assumed in the analysis to 
    922 lbs per basket.
        The revised containment analysis shows that using an average 
    basket weight of 1,071 lbs and a sublimation allowance of 15 
    percent, all bays would have an average basket weight of 922 lbs at 
    the end of the 18-month surveillance interval. The revised analysis 
    utilizes new mass and energy releases (refer to Westinghouse WCAP-
    10325-P-A), which substantially delays ice-bed meltout and limits 
    the initial containment peak pressure to approximately 7.15 psig 
    during the blowdown phase. The ice-bed meltout delay allows the 
    second containment pressure peak, which is driven mainly by the 
    decay heat, to be limited to approximately 11.45 psig, which is 
    below the containment design pressure of 12 psig.
        Based on TVA's evaluation and the revised containment analysis, 
    TVA considers the reduction of the average basket weight to be 
    acceptable for satisfying the safety function of the ice condenser 
    for the current 18-month interval. Therefore, the proposed change 
    does not involve a significant reduction in the margin of safety.
        The proposal to extend the surveillance from 12 to 18 months 
    does not change the boron concentration or pH requirements. 
    Experience at Duke Power Company, as stated in NUREG-1366, indicates 
    that these parameters do not change appreciably when verified every 
    9 months. SQN has a similar experience with a 12-month interval. 
    Since the boron concentration and the post-LOCA pH requirements 
    remain essentially the same, there is no reduction in the margin of 
    safety.
        Elimination of the temperature at which the pH of the ice bed is 
    determined is an administrative change. Future testing will be 
    accomplished in accordance with ASTM recommendations. The difference 
    between the pH values determined at the current TS specified 
    temperature and the temperature currently recommended by the ASTM 
    standards is insignificant. Therefore, there is no reduction in the 
    margin of safety.
        The NRC has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: September 12, 1996
        Description of amendment request: The proposed change to the 
    Technical Specifications is administrative in nature in that it would 
    add the NRC standard fire protection license condition to each unit's 
    Operating License and relocate the fire protection requirements from 
    the Technical Specifications to the Updated Final Safety Analysis 
    Report (UFSAR).
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    [[Page 19836]]
    
        Specifically, operation of Surry Power Station with the proposed 
    amendment will not:
        1. Involve a significant increase in either the probability of 
    occurrence or consequences of any accident or equipment malfunction 
    scenario that is important to safety and which has been previously 
    evaluated in the UFSAR. The requirements of the Fire Protection 
    Program have not been changed by theproposed amendment. Relocation 
    of the Fire Protection Program requirements into the UFSAR and 
    station procedures does not decrease any portion of the program. The 
    same fire protection requirements exist as before the change.
        2. Create the possibility of a new or different type of accident 
    than those previously evaluated in the safety analysis report. The 
    requirements of the Fire Protection Program have not been changed by 
    the proposed amendment. This is an administrative change to relocate 
    the Fire Protection Program requirements from the Technical 
    Specifications to the UFSAR and station procedures. Consequently, 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated has not been created.
        3. Involve a significant reduction in a margin of safety. 
    Implementation of the Fire Protection Program requirements is 
    assured by the UFSAR and station procedures. Since the rogram is 
    being retained intact, there is no reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219
        NRC Project Director: Mark Reinhart, Acting
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: January 16, 1997
        Description of amendment request: The proposed amendments (Point 
    Beach Nuclear Plant (PBNP) Technical Specifications (TS) Change Request 
    (TSCR) 191) would revise the minimum boron concentration required in 
    the refueling water storage tank(s)(RWST), boric acid storage tanks 
    (BAST), and safety injection (SI) accumulators during normal operation; 
    the minimum boron concentration of primary coolant during refueling 
    conditions; and the minimum boron concentration in the reactor when 
    positive reactivity could be added and/or boron dilution could occur 
    and containment integrity is not intact. These changes are necessary to 
    accommodate the planned extension of the operating cycle from 12 months 
    to 18 months. The licensee proposes to change TS 15.3.2, ``Chemical and 
    Volume Control System,'' TS 15.3.3, ``Safety Injection and Residual 
    Heat Removal Systems,'' TS 15.3.6, ``Containment System,'' TS 15.3.8, 
    ``Refueling,'' and associated Bases.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of this facility under the proposed Technical 
    Specifications will not create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The probabilities of accidents previously evaluated are based on 
    the probability of initiating events for these accidents. Initiating 
    events for accidents previously evaluated are described in the PBNP 
    FSAR [final safety analysis report].
        In effect, the proposed changes will result in: (1) higher boron 
    concentrations of primary coolant during refueling, and (2) higher 
    boron inventories in the RWSTs, BASTs, and SI accumulators. These 
    changes do not require hardware changes or changes to the operation 
    of accident-mitigating equipment. These changes relate to the 
    performance capability of particular accident mitigation systems; 
    equipment that is not postulated to cause accidents. Therefore, 
    these proposed changes do not cause an increase in the probabilities 
    of any accidents previously evaluated.
        The consequences of accidents previously evaluated in the PBNP 
    FSAR are determined by the results of analyses that are based on 
    initial conditions of the plant, the type of accident, transient 
    response of the plant, and the operation and failure of equipment 
    and systems.
        In effect, the proposed changes will result in: (1) higher boron 
    concentrations of primary coolant during refueling, and (2) higher 
    boron inventories in the RWSTs, BASTs, and SI accumulators. These 
    increased boron concentrations do not increase the probability that 
    engineered safety features equipment will fail, nor do these changes 
    affect the capability of this equipment to operate as required for 
    the accidents previously evaluated in the PBNP FSAR. These changes 
    do not require hardware changes or changes to the operation of 
    accident-mitigating equipment.
        The consequential effects of a lower containment spray pH will 
    not affect the capability of the containment spray to remove 
    elemental iodine during design basis LOCA [loss-of-coolant accident] 
    accidents. Also, the consequential reduction in containment sump 
    water pH will not affect the fluid's capability to retain elemental 
    iodine, nor will it adversely increase the potential corrosion rates 
    for materials inside containment if the sump water is sprayed into 
    containment during the recirculation phase of a LOCA.
        Another consequence of injecting a higher concentration boric 
    acid solution into the core during a LOCA may be an abbreviated 
    onset to boron precipitation in the post-LOCA core. An incremental 
    change in the boron injection concentration would not have 
    significant effect on the postulated onset, but each core reload 
    safety evaluation will continue to verify that the existing 
    emergency operating procedures accommodate the potential for boron 
    precipitation.
        Therefore, this proposed license amendment does not affect the 
    consequences of any accident previously evaluated in the PBNP FSAR, 
    because the factors that are used to determine the consequences of 
    accidents are not changed.
        2. Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        New or different kinds of accidents can only be created by new 
    or different accident initiators or sequences. New and different 
    types of accidents (different from those that were originally 
    analyzed for Point Beach) have been evaluated and incorporated into 
    the licensing basis for PBNP. Examples of different accidents that 
    have been incorporated into the PBNP licensing basis include 
    anticipated transients without scram and station blackout.
        The changes proposed by this TSCR do not create any new or 
    different accident initiators or sequences because these changes to 
    minimum boron concentrations will not cause failures of equipment or 
    accident sequences different than the accidents previously analyzed. 
    No new equipment interfaces are created, and no new materials or 
    fluids are introduced. The incremental increase in boron 
    concentrations will not create a failure mechanism not previously 
    known and evaluated. Therefore, these proposed TS changes do not 
    create the possibility of an accident of a different type than any 
    previously evaluated in the PBNP FSAR.
        3. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The margins of safety for Point Beach are based on the design 
    and operation of the reactor and containment and the safety systems 
    that provide their protection. Plant safety margins are established 
    through Limiting Conditions for Operation, Limiting Safety System 
    Settings and Safety Limits specified in the Technical 
    Specifications. The proposed Technical Specification changes to 
    refueling water storage tank (RWST), SI accumulator, and BAST boron 
    inventory requirements have all been evaluated to preserve the 
    shutdown capability described in the associated bases (boration from 
    just critical, hot zero or full power, peak xenon with control rods 
    at the
    
    [[Page 19837]]
    
    insertion limit, to xenon-free cold shutdown with the highest worth 
    control rod assembly fully withdrawn). Similarly, the proposed TS 
    change to the minimum boron concentration of the primary coolant 
    system for refueling operations have been evaluated to preserve the 
    subcriticality margin described in the associated TS bases (i.e., 5% 
    [delta] k/k in the cold condition with all rods inserted).
        Because there are no changes to any of these margins, the 
    proposed license amendment does not involve a reduction in any 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: January 21, 1997
        Description of amendment request: The proposed amendments (Point 
    Beach Nuclear Plant (PBNP) Technical Specifications (TS) Change Request 
    195) would revise TS Section 15.6.11, ``Radiation Protection Program,'' 
    to update all references to 10 CFR Part 20, ``Standards for Protection 
    Against Radiation,'' to restore consistency between 10 CFR Part 20 
    regulations and the PBNP TS.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed amendments are administrative in nature, providing 
    consistency between the Point Beach licenses and Commission 
    regulations. The amendments do not affect the operation or 
    maintenance of any PBNP structure[,] system or component. In 
    addition, the regulations and proposed changes provide more 
    conservative determinations of high radiation areas, thereby 
    potentially resulting in lower personnel radiation exposures during 
    normal operation and post accident. The consequences of an accident 
    related to personnel radiation exposures may be reduced.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed amendments are administrative only and do not 
    affect the operation or maintenance of any structure[,] system or 
    component at Point Beach Nuclear Plant. No new systems or components 
    are introduced. Therefore, no new accident initiators or sequences 
    result from any previously evaluated.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create a significant reduction in a 
    margin of safety.
        The proposed amendments are administrative and reflect 
    regulatory requirements that are more conservative than those 
    presently reflected in the PBNP Technical Specifications. These more 
    conservative requirements result in more conservative designation of 
    high radiation areas thereby providing additional margins of safety 
    related to the control of radiation exposures to personnel. No 
    structure[,] system or component at PBNP at PBNP is changed[,] 
    thereby maintaining the margins of safety for the operation of the 
    Point Beach Nuclear Plant.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: January 24, 1997
        Description of amendment request: The proposed amendments (Point 
    Beach Nuclear Plant (PBNP) Technical Specifications (TS) Change Request 
    (TSCR) 193) would revise TS 15.5.4, ``Fuel Storage,'' to increase fuel 
    assembly enrichment limits to 5.0 w/o U-235 while maintaining Keff in 
    the storage pools (spent fuel pool and new fuel storage racks) less 
    than 0.95.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of this facility under the proposed Technical 
    Specifications will not create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes do not involve a change to structures, 
    systems, or components which would affect the probability or 
    consequences of an accident previously evaluated in the PBNP Final 
    Safety Analysis Report (FSAR). The only relevant concern with 
    respect to increasing enrichment limits in the spent fuel pool and 
    new fuel storage racks is one of criticality. The proposed changes 
    use the same criticality limit used in the current Technical 
    Specifications. Therefore, margin to safe operation of Units 1 and 2 
    is maintained. The probability and consequences of an accident 
    previously evaluated are dependent on this criticality limit. 
    Because the limit will not change, the probability and consequences 
    of those accidents previously evaluated will not change.
        2. Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not involve a change to plant design. 
    The proposed increase in spent fuel pool and new fuel storage racks 
    fuel assembly enrichment limits maintains the margin to safe 
    operation of Units 1 and 2 because the criticality limit for the 
    spent fuel pool and new fuel storage racks will not change. These 
    changes do not affect any of the parameters or conditions that 
    contribute to the initiation of any accidents. Because the 
    criticality limit remains the same, these changes have no effect on 
    plant operation, design, or initiation of any accidents. Therefore, 
    the proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The proposed changes maintain the margin to safe operation of 
    Units 1 and 2. The margin of safety is based on the criticality 
    limit of the spent fuel pool and the new fuel storage racks. Because 
    this limit will not change, the margin of safety will not be 
    affected. Therefore, the proposed changes will not create a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
    
    [[Page 19838]]
    
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: February 12, 1997, as supplemented on 
    March 11, 1997
        Description of amendment request: The proposed amendments (Point 
    Beach Nuclear Plant (PBNP) Technical Specifications (TS) Change Request 
    196) would relocate turbine overspeed protection specifications, 
    limiting conditions for operation, surveillance requirements, and 
    associated bases from TS Section 15.3.4, ``Steam and Power Conversion 
    System,'' and Section 15.4.1, ``Operational Safety Review,'' to the 
    Final Safety Analysis Report (FSAR) in accordance with Generic Letter 
    95-10, ``Relocation of Selected Technical Specifications Requirements 
    Related to Instrumentation.''
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of Point Beach Nuclear Plant in accordance with the 
    proposed amendments will not result in a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments administratively relocate turbine 
    overspeed protection Specifications to the Point Beach Final Safety 
    Analysis Report (FSAR). The Specifications will be transferred 
    verbatim, except for the turbine load limit with the crossover steam 
    dump system inoperable, which has already been evaluated under 10 
    CFR 50.59 and will be conservatively reduced. In addition, the 
    regulatory requirements of 10 CFR 50.55a, ``Codes and Standards, '' 
    will still apply to the relocated Specifications. Therefore, 
    operation of Point Beach Nuclear Plant in accordance with the 
    proposed amendments cannot create an increase in the probability or 
    consequences of an accident previously evaluated.
        2. Operation of Point Beach Nuclear Plant in accordance with the 
    proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed amendments administratively relocate Specifications 
    to the FSAR and in one case result in a more conservative operating 
    limit. Therefore, operation of Point Beach Nuclear Plant in 
    accordance with the proposed amendments cannot create a new or 
    different kind of accident from any accident previously evaluated.
        3. Operation of Point Beach Nuclear Plant in accordance with the 
    proposed amendments will not create a significant reduction in a 
    margin of safety.
        The proposed changes are administrative in nature. There is no 
    physical change to the facility, its systems, or its operation, 
    except for the conservative reduction of the turbine load limit with 
    the crossover steam dump system inoperable which has already been 
    justified via 10 CFR 50.59. Therefore, operation of PBNP in 
    accordance with the proposed amendments cannot result in a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: February 17, 1997; supersedes March 24, 
    1995, as supplemented by letter dated August 16, 1995, amendment 
    request.
        Description of amendment request: This amendment request proposes 
    to revise Technical Specification 1.7, ``Containment Integrity,'' 
    Technical Specification 3/4.6.1, ``Containment Integrity,'' and 
    Technical Specification 3/4.6.3, ``Containment Isolation Valves.'' 
    These proposed changes would relocate Technical Specification Table 
    3.6-1, ``Containment Isolation Valves,'' to the Wolf Creek Generating 
    Station (WCGS) procedures. This proposed change is in accordance with 
    the guidance provided in Generic Letter 91-08, ``Removal of Component 
    Lists from Technical Specifications,'' dated May 6, 1991. In addition, 
    this request proposes that the August 16, 1996, supplemental submittal 
    that provided an additional footnote allowing an increased outage time 
    for certain component cooling water system valves be withdrawn. The 
    determination that the additional footnote is not required supersedes 
    the staff's proposed no significant hazards consideration determination 
    evaluation for the requested changes that was published on September 
    27, 1995 (60 FR 49949).
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes simplify the technical specifications, meet 
    the regulatory requirements for control of containment isolation, 
    and are consistent with the guidelines of GL 91-08. The procedural 
    details of Technical Specification Table 3.6-1 have not been 
    changed, but only relocated to a different controlling document. The 
    proposed changes are administrative in nature, should result in 
    improved administrative practices, and do not affect plant 
    operations.
        The probability of occurrence of a previously evaluated accident 
    is not increased because this change does not introduce any new 
    potential accident initiating conditions. The consequences of an 
    accident previously evaluated is not increased because the ability 
    of containment to restrict the release of any fission product 
    radioactivity to the environment will not be degraded by this 
    change.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are administrative in nature, do not result 
    in physical alterations or changes to the operation of the plant, 
    and cause no change in the method by which any safety-related system 
    performs its function. Therefore, this proposed change will not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The administrative change to relocate Technical Specification 
    Table 3.6-1 to appropriate plant procedures does not alter the basic 
    regulatory requirements for containment isolation and will not 
    adversely affect containment isolation capability for Coordinator 
    credible accident scenarios. Adequate control of the content of the 
    table is assured by existing plant procedures.
        The proposed relocation of Technical Specification Table 3.6-1 
    does not alter current technical specification requirements for 
    containment isolation valve operability. The LCO and Surveillance 
    Requirements would be retained in the revised technical 
    specifications. Therefore, the proposed change will not affect the 
    meaning, application, and function of the current technical 
    specification requirements for the valves in Table 3.6-1.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
    [[Page 19839]]
    
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 18, 1997
        Description of amendment request: This license amendment request 
    revises Technical Specification Surveillance Requirement 4.5.2.c to 
    clarify when a containment entry visual inspection is required. This 
    proposed change to reduce the visual inspection requirement to at least 
    once daily is in accordance with the guidance provided in Generic 
    Letter 93-05, ``Line-Item Technical Specifications Improvements to 
    Reduce Surveillance Requirements for Testing During Power Operation.''
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Implementing the proposed change could potentially increase the 
    chances of loose debris (trash, rags, clothing, etc.) being left in 
    containment for some period of time greater than would be allowed 
    under current surveillance requirements. However, the proposed 
    change also clarifies that the visual inspection must be performed 
    at least once daily. Therefore, the period of time that debris could 
    be left uncontrolled inside containment would still be less than 24 
    hours. Based on work controls placed on material entry/exit into 
    containment and personnel training on housekeeping controls inside 
    containment, and the results of past surveillances, it is unlikely 
    that a significant amount of debris would be left uncontrolled 
    inside containment for this period of time. Also, based on 
    containment sump design, relatively small amounts of debris would 
    not be sufficient to cause a significant amount of blockage of the 
    sump screens.
        The probability of occurrence of a previously evaluated accident 
    is not increased because the reduced frequency of the visual 
    inspection does not cause a significant impact on the possibility of 
    containment sump screen blockage. Therefore containment sump 
    operability is not affected by the proposed change. In addition, the 
    proposed change will not result in any changes to the design or 
    operation of any plant systems or components.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change decreases the frequency of performing a 
    visual inspection for loose debris in containment, but does not 
    result in a change to the design or operation of any plant system or 
    component. The purpose of the inspection is to ensure that there is 
    no loose debris, left in containment following a containment entry, 
    that could potentially block the containment sump screens during 
    LOCA conditions. Delaying this inspection until the last containment 
    entry each day will not result in a significant amount of debris 
    being left in containment, based on housekeeping practices 
    controlling the entry/removal of trash and material into/from 
    containment; training of employees to increase awareness of material 
    control in radiologically-controlled areas; and retaining the 
    requirement to perform a visual inspection at least once per day 
    when containment entries are made (during periods when containment 
    integrity is established), thereby ensuring that trash and debris 
    can be identified and removed on a daily basis (on days containment 
    entries are made).
        Based on the above, this proposed change will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The purpose of performing a visual inspection of areas affected 
    by a containment entry is to ensure any debris or trash generated by 
    the activity during the containment entry is identified and removed 
    from containment. This ensures that no trash or debris is left in 
    containment that could be transported to and block the containment 
    sump screens during LOCA conditions. Based on current material 
    control and housekeeping practices imposed on containment entry/
    exit, and past inspection results, reducing the surveillance 
    requirement to a once per day basis, on days containment entries are 
    made, would not result in a significant amount of trash or debris 
    being left in containment following completion of the entry, and any 
    such material would be identified and removed prior to the end of 
    the day. The amount of trash or debris that could be left in 
    containment for a 24 hour period would be significantly less than 
    the amount that would be required to cause sump screen blockage 
    sufficient to affect sump performance. Therefore, the proposed 
    change will not result in a significant reduction in the margin of 
    safety of any plant system or equipment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 18, 1997
        Description of amendment request: This license amendment request 
    revises Technical Specification Section 5.3.1, Fuel Assemblies, to 
    allow the use of an alternate zirconium based fuel cladding material, 
    ZIRLO. Wolf Creek Nuclear Operating Corporation (WCNOC) is planning to 
    insert Westinghouse fuel assemblies containing ZIRLO fuel rod cladding 
    during the ninth refueling outage, which is currently scheduled to 
    begin in late September 1997.
        Basis for proposed no significant Hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The methodologies used in the accident analysis remain 
    unchanged. The proposed changes do not change or alter the design 
    assumptions for the systems or components used to mitigate the 
    consequences of an accident. Use of ZIRLO fuel cladding does not 
    adversely affect fuel performance or impact nuclear design 
    methodology. Therefore accident analyses are not impacted.
        The operating limits will not be changed and the analysis 
    methods to demonstrate operation within the limits will remain in 
    accordance with NRC approved methodologies. Other than the changes 
    to the fuel assemblies, there are no physical changes to the plant 
    associated with this technical specification change. A safety 
    analysis will continue to be performed for each cycle to demonstrate 
    compliance with all fuel safety design basis.
        VANTAGE 5H with IFMs fuel assemblies with ZIRLO clad fuel rods 
    meet the same fuel assembly and fuel rod design bases as other 
    VANTAGE 5H with IFMs fuel assemblies. In addition, the 10 CFR 50.46 
    criteria are applied to the ZIRLO clad rods. The use of these fuel 
    assemblies will not result in a change to the reload design and 
    safety analysis limits. The clad material is similar
    
    [[Page 19840]]
    
    in chemical composition and has similar physical and mechanical 
    properties as Zircaloy-4. Thus, the cladding integrity is maintained 
    and the structural integrity of the fuel assembly is not affected. 
    ZIRLO cladding improves corrosion performance and dimensional 
    stability. No concerns have been identified with respect to the use 
    of an assembly containing a combination of Zircaloy-4 and ZIRLO clad 
    fuel rods. Since the dose predictions in the safety analyses are not 
    sensitive to fuel rod cladding material, the radiological 
    consequences of accidents previously evaluated in the safety 
    analysis remain valid.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident or 
    malfunction of equipment important to safety previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        VANTAGE 5H with IFMs fuel assemblies with ZIRLO clad fuel rods 
    satisfy the same design bases as those used for other VANTAGE 5H 
    with IFMs fuel assemblies. All design and performance criteria 
    continue to be met and no new failure mechanisms have been 
    identified. Since the original design criteria are met, the ZIRLO 
    clad fuel rods will not be an initiator for any new accident or 
    malfunction of equipment important to safety. The ZIRLO cladding 
    material offers improved corrosion resistance and structural 
    integrity.
        The proposed changes do not affect the design or operation of 
    any system or component in the plant. The safety functions of the 
    related structures, systems or components are not changed in any 
    manner, nor is the reliability of any structure, system or component 
    reduced. The changes do not affect the manner by which the facility 
    is operated and do not change any facility design feature, structure 
    or system. No new or different type of equipment will be installed. 
    Since there is no change to the facility or operating procedures, 
    and the safety functions and reliability of structures, systems and 
    components are not affected, the proposed changes do not create the 
    possibility of a new or different kind of accident or malfunction of 
    equipment important to safety from any accident or malfunction of 
    equipment important to safety previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Use of ZIRLO cladding material does not change the VANTAGE 5H 
    with IFMs reload design and safety limits. The use of these fuel 
    assemblies will take into consideration the normal core operating 
    conditions allowed in the Technical Specifications. For each cycle 
    reload core, the fuel assemblies will be evaluated using NRC 
    approved reload design methods, including consideration of the core 
    physics analysis peaking factors and core average linear heat rate 
    effects.
        The use of Zircaloy-4, ZIRLO or stainless steel filler rods in 
    fuel assemblies will not involve a significant reduction in the 
    margin of safety because analyses using NRC approved methodologies 
    will be performed for each configuration to demonstrate continued 
    operation within the limits that assure acceptable plant response to 
    accidents and transients. These analyses will be performed using NRC 
    approved methods that have been approved for application to the fuel 
    configuration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: March 27, 1997
        Description of amendments request: The proposed amendments would 
    revise the Technical Specifications for the Brunswick Steam Electric 
    Plant Units 1 and 2 to eliminate certain instrumentation response time 
    testing requirements in accordance with NRC-approved BWR Owners Group 
    Topical Report NEDO-32291-A, ``System Analysis for the Elimination of 
    Selected Response Time Testing Requirements.''Date of publication of 
    individual notice in Federal Register: April 1, 1997 (62 FR 15542)
        Expiration date of individual notice: May 1, 1997
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297
    
    Southern Nuclear Operating Company, Inc., Docket No. 50-348, Joseph 
    M. Farley Nuclear Plant, Unit No. 1, Houston County, Alabama
    
        Date of amendment request: March 25, 1997
        Description of amendment request: The proposed amendment would 
    modify Technical Specification 3/4.4.9, ``Specific Activity,'' and 
    associated Bases to reduce the limit associated with dose equivalent 
    iodine-131. The steady-state dose equivalent iodine-131 limit would be 
    reduced by 40 percent from .5 [micro]Curie/gram to .3 [micro]Curie/
    gram.
        Date of publication of individual notice in Federal Register: April 
    4, 1997 (62 FR 16201)
        Expiration date of individual notice: May 5, 1997
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental
    
    [[Page 19841]]
    
    assessment need be prepared for these amendments. If the Commission has 
    prepared an environmental assessment under the special circumstances 
    provision in 10 CFR 51.12(b) and has made a determination based on that 
    assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of application for amendments: February 19, 1997, as 
    supplemented April 3, 1997.
        Brief description of amendments: The amendments would delete the 
    24/48 Volt direct current (Vdc), batteries, battery chargers and 
    distribution systems from the Technical Specifications (TSs) for Unit 
    3, by adding a footnote to indicate that these TSs are only applicable 
    to Unit 2. All safety-related loads associated with the 24/48 Vdc 
    batteries for Unit 3 will be relocated to other safety-related battery 
    systems which are in the TSs.
        Date of issuance: April 10, 1997
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 156 and 151
        Facility Operating License Nos. DPR-19 and DPR-25: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 5, 1997 (62 FR 
    10088). The April 3, 1997, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    April 10, 1997. No significant hazards consideration comments received: 
    No
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: August 14, 1996, as supplemented 
    September 13, 1996
        Brief description of amendment: The amendment revises Technical 
    Specification Sections 3.3 and 6.9.1.9; and the basis of Section 3.3, 
    3.6 and 3.10. The changes incorporate the best estimate approach into 
    the licensing basis for the Indian Point Unit No. 2 loss-of-coolant 
    accident analysis.
        Date of issuance: March 31, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 188
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4344) The September 13, 1996, supplemental letter did not change the 
    initial proposed no significant hazards consideration.The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated March 31, 1997.No significant hazards consideration comments 
    received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: February 14, 1997, as 
    supplemented March 12, 1997.
        Brief description of amendment: The amendment revises Technical 
    Specification Section 4.13-2 to allow a one-time extension of the 
    interval for steam generator tube inspection. Specifically, the date 
    for commencement of the steam generator tube inspection is extended 
    from April 14, 1997 to May 2, 1997.
        Date of issuance: April 9, 1997
        Effective date: As of the date of issuance to be implemented by 
    April 14, 1997.
        Amendment No.: 189
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 4, 1997 (62 FR 
    9816) The March 12, 1997, supplemental letter provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated April 9, 1997.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of application for amendment: November 7, 1996
        Brief description of amendment: The amendment revised Technical 
    Specification 4.2.9, Service and Instrument Air System, to add an 
    additional air compressor.
        Date of issuance: April 2, 1997
        Effective date: Effective the date of issuance.
        Amendment No.: 118
        Facility Operating License No. DPR-6: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 18, 1996 (61 
    FR 66706) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 2, 1997.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: January 3, 1997, as 
    supplemented by letter dated March 20, 1997
        Brief description of amendments: The amendments revise Technical 
    Specification Tables 3.3-2, 3.3-4, 3.3-5, 4.3-2 and Bases Sections 3/
    4.3.1 and 3/4.3.2 to eliminate the safety injection signal on low steam 
    line pressure.
        Date of issuance:  April 3, 1997
        Effective date: For Unit 1, as of the date of issuance to be 
    implemented before startup from the next refueling outage; For Unit 2, 
    as of the date of issuance to be implemented before startup from the 
    current refueling outage
        Amendment Nos.: 158 and 150
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4345) The March 20, 1997, letter provided clarifying information that 
    did not change the scope of the original January 3, 1997, application 
    and the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated April 3, 1997.No significant hazards 
    consideration comments received: No
    
    [[Page 19842]]
    
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application for amendments: February 5, 1997
        Brief description of amendments: The amendments reflect replacement 
    of the existing source and intermediate range nuclear instrumentation 
    with a new source range and wide range nuclear instrumentation system 
    that provides more channels and continuous coverage from the Source 
    Range to above the Power Range.
        Date of issuance: March 31, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 223, 223, 220
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8796) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 31, 1997.No significant 
    hazards consideration comments received:
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: October 16, 1996
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications by revising Table 4.3-1 to expand the 
    applicability for Core Protection Calculator (CPC) operability and to 
    allow the use of a cycle independent shape annealing matrix in the 
    CPCs.
        Date of issuance: April 11, 1997
        Effective date: April 11, 1997, to be implemented within 60 days
        Amendment No.: 125
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6575) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 11, 1997No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: December 2, 1996 as supplemented by 
    letter dated February 4 and March 14, 1997
        Brief description of amendment: The amendment changes the Technical 
    Specifications to reflect the approval for the licensee to use of the 
    new Containment Leakage Rate Testing Program as required by 10 CFR Part 
    50 Appendix J, Option B for Waterford Steam Electric Station, Unit 3.
        Date of issuance: April 10, 1997
        Effective date: April 10, 1997
        Amendment No.: 124
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 15, 1997 (62 FR 
    2189) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 10, 1997.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    Florida Power and Light Company, et al., Docket No. 50-335, St. 
    Lucie Plant, Unit No. 1, St. Lucie County, Florida
    
        Date of application for amendment: December 9, 1996
        Brief description of amendment: This amendment modifies technical 
    specifications for selected cycle-specific reactor physics parameters 
    to refer to the St. Lucie Unit 1 Core Operating Limits Report for 
    limiting values.
    
        Date of issuance:  April 1, 1997
        Effective date: April 1, 1997
        Amendment No.: 150
        Facility Operating License No. NPF-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 15, 1997 (62 FR 
    2189) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 1, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of applications for amendment: June 20, 1995, as supplemented 
    August 30, 1995, and January 17, 1996
        Brief description of amendment: The amendment relocates the 
    applicable requirements of Technical Specification (TS) 3.6.3 for the 
    main steam line isolation valves (MSIVs) to TS 3.7.1.5, ``Main Steam 
    Line Isolation Valves.'' In addition, the Applicability section of TS 
    3.7.1.5 is revised to indicate that Specification 3.7.1.5 is applicable 
    in Mode 1 and in Modes 2, 3, and 4, except where all MSIVs are closed 
    and deactivated (i.e., in Modes 2, 3, and 4, TS 3.7.1.5 is applicable 
    only if the MSIVs are open). Also, the Action Statement for the 
    Limiting Condition for Operation 3.7.1.5 has been revised using the 
    guidance of the Improved Standard Technical Specifications for 
    Westinghouse plants (NUREG-1431). The amendment also deletes a license 
    requirement to submit responses to and to implement requirements of 
    Generic Letter 83-28, because the requirement has been completed. 
    Generic Letter 83-28 pertains to the Salem anticipated transient 
    without scram event. In addition, the amendment incorporates TS Bases 
    submitted by Northeast Nuclear Energy Company by letters dated June 20, 
    1995, February 5, 1996, and March 21 and 26, 1997. Since all four Bases 
    changes affect Section B 3/4.7 of the TS, the NRC staff is using them 
    in a group to avoid errors in revising the TS.
        Date of issuance: April 10, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 136
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications and License Condition.
        Date of initial notice in Federal Register: August 2, 1995 (61 FR 
    39445) and February 28, 1996 (61 FR 7555)The August 30, 1995, letter 
    provided clarifying information that did not change the scope of the 
    June 20, 1995, application and the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 10, 1997.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike,
    
    [[Page 19843]]
    
    Norwich, Connecticut and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, Connecticut 06385
    
    Northeast Nuclear Energy Company, et al., Docket Nos. 50-245, 50-
    336, and 50-423, Millstone Nuclear Power Station, Unit Nos. 1, 2, 
    and 3, New London, Connecticut
    
        Date of application for amendments: February 3, 1997
        Brief description of amendments: The amendments revise Section 6, 
    ``Administrative Controls,'' of the Millstone Unit Nos. 1, 2, and 3 
    Technical Specifications to reflect organizational changes that have 
    been implemented in the Nuclear Division.
        Date of issuance: April 10, 1997
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment Nos.: 99, 206, and 135
        Facility Operating License Nos. DPR-21, DPR-65, and NPF-49: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8800) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 10, 1997.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: November 18, 1996
        Brief description of amendments: These amendments change the 
    Technical Specifications for Susquehanna Steam Electric Station (SSES), 
    Units 1 and 2 by increasing the maximum isolation times for reactor 
    core isolation cooling inboard warm-up line isolation valves from 3 
    seconds to 12 seconds, high pressure core injection inboard warm-up 
    line siolation valves from 3 seconds to 6 seconds and reactor 
    recirculation process sample line isolation valves from 2 seconds to 9 
    seconds.
        Date of issuance: April 7, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 164 and 135
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 15, 1997 (61 FR 
    2191) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 7, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Pennsylvania Power and Light Company, Docket No. 50-388, 
    Susquehanna Steam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendment:  March 17, 1997
        Brief description of amendment: The amendment modifies the Design 
    Features Section 5.3.1 of the Technical Specifications to reflect the 
    Atrium-10 design and would include a Siemens Power Corporation topical 
    report in Section 6.9.3.2 to reflect mechanical design criteria for 
    this fuel. This change would allow this fuel to be loaded into the core 
    only under Operational Condition 5 (refueling) and does not permit 
    startup or power operation using the Atrium-10 fuel.
        Date of issuance: April 9, 1997
        Effective date: As of date of issuance to be implemented within 30 
    days.
        Amendment No.: 136
        Facility Operating License No. NPF-22: This amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes (62 FR 14167) March 25, 1997. 
    That notice provided an opportunity to submit comments on the 
    Commission's proposed no significant hazards consideration 
    determination. No comments have been received. The notice also provided 
    for an opportunity to request a hearing by April 24, 1997, but 
    indicated that if the Commission makes a final no significant hazards 
    consideration determination any such hearing would take place after 
    issuance of the amendment. The Commission's related evaluation of the 
    amendment, finding of exigent circumstances, and final determination of 
    no significant hazards consideration are contained in a Safety 
    Evaluation dated April 9, 1997.
        Attorney for licensee: Jay Silbert, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington DC 20037.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, 
    Edwin I. Hatch Nuclear Plant, Units 1 and 2, Appling County, 
    Georgia
    
        Date of application for amendments: September 19, 1996, as 
    supplemented December 17, 1996, January 23 and 31, March 21 and April 
    4, 1997
        Brief description of amendments: The amendments revise the 
    surveillance requirements addressing the reactor vessel pressure and 
    temperature limits.
        Date of issuance: April 4, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 206 and 147
        Facility Operating
        Local Public- Document -Room locations: ments revised the Technical 
    Specifications.
        Date of initial notice in Federal Register: January 2, 1997 (62 FR 
    128) The December 17, 1996, January 23 and 31, March 21, 1997, and 
    April 4, 1997, letters provided clarifying information that did not 
    change the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated April 4, 1997.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: October 18, 1996 as 
    supplemented March 12, March 17, April 4, and April 9, 1997 (TS 96-05)
        Brief description of amendments: The amendments change the 
    Technical Specifications (TS) by revising TS 3/4.4.5 and 3.4.6.2 and 
    associated Bases to permanently incorporate requirements for steam 
    generator tube inspections and repair in the Sequoyah Nuclear Plant, 
    Units 1 and 2 TS.
        Date of issuance: April 9, 1997
        Effective date: As of the date of issuance to be implemented no 
    later than 45 days of its issuance.
        Amendment Nos.: 222 and 213
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications and license conditions.
    
    [[Page 19844]]
    
        Date of initial notice in Federal Register: February 11, 1997 (62 
    FR 6276) The March 12, March 17, April 4, and April 9, 1997, letters 
    provided clarifying information that did not change the scope of the 
    October 18, 1996, application and the initial proposed no significant 
    hazards consideration determination.The Commission's related evaluation 
    of the amendment is contained in a Safety Evaluation dated April 9, 
    1997.No significant hazards consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By May 23, 1997, the licensee 
    may file a request for a hearing with respect to issuance of the 
    amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order. required by 10 CFR 2.714, a petition for leave to 
    intervene shall set forth with particularity the interest of the 
    petitioner in the proceeding, and how that interest may be affected by 
    the results of the proceeding. The petition should specifically explain 
    the reasons why intervention should be permitted with particular 
    reference to the following factors: (1) the nature of the petitioner's 
    right under the Act to be made a party to the proceeding; (2) the 
    nature and extent of the petitioner's property, financial, or other 
    interest in the proceeding; and (3) the possible effect of any order 
    which may be entered in the proceeding on the petitioner's interest. 
    The petition should also identify the specific aspect(s) of the subject 
    matter of the proceeding as to which petitioner wishes to intervene. 
    Any person who has filed a petition for leave to intervene or who has 
    been admitted as a party may amend the petition without requesting 
    leave of the Board up to 15 days prior to the first prehearing 
    conference scheduled in the proceeding, but such an amended petition 
    must satisfy the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a
    
    [[Page 19845]]
    
    supplement to the petition to intervene which must include a list of 
    the contentions which are sought to be litigated in the matter. Each 
    contention must consist of a specific statement of the issue of law or 
    fact to be raised or controverted. In addition, the petitioner shall 
    provide a brief explanation of the bases of the contention and a 
    concise statement of the alleged facts or expert opinion which support 
    the contention and on which the petitioner intends to rely in proving 
    the contention at the hearing. The petitioner must also provide 
    references to those specific sources and documents of which the 
    petitioner is aware and on which the petitioner intends to rely to 
    establish those facts or expert opinion. Petitioner must provide 
    sufficient information to show that a genuine dispute exists with the 
    applicant on a material issue of law or fact. Contentions shall be 
    limited to matters within the scope of the amendment under 
    consideration. The contention must be one which, if proven, would 
    entitle the petitioner to relief. A petitioner who fails to file such a 
    supplement which satisfies these requirements with respect to at least 
    one contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: April 1, 1997
        Brief description of amendment: The amendment revises Technical 
    Specification Table 3.3-3 to correct administrative errors associated 
    with the start logic of the turbine driven auxiliary feedwater pump.
        Date of issuance: April 2, 1997
        Effective date: April 2, 1997
        Amendment No.: 119
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No.The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated April 2, 1997.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, NW., Washington, DC 200379
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
        NRC Project Director: William H. Bateman
        Dated at Rockville, Maryland, this 16th day of April, 1997.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director ,Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation
    [Doc. 97-10334 Filed 4-22-97; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
04/23/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X97-10423
Dates:
Immediately, to be implemented within 30 days.
Pages:
19825-19845 (21 pages)
PDF File:
x97-10423.pdf