99-10685. St. Lucie Plant, Unit 2 Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 64, Number 82 (Thursday, April 29, 1999)]
    [Notices]
    [Pages 23133-23136]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-10685]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Florida Power & Light Company, Inc.
    [Docket No. 50-389]
    
    
    St. Lucie Plant, Unit 2 Environmental Assessment and Finding of 
    No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (NRC or the Commission) is 
    considering issuance of an amendment to Facility Operating License No. 
    NPF-16, issued to Florida Power & Light Company, Inc., (the licensee), 
    for operation of the St. Lucie Plant, Unit 2, located in St. Lucie 
    County, Florida.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed amendment would modify the St. Lucie Plant, Unit 2, 
    Technical Specifications by changing the criticality requirements for 
    the design of the spent fuel storage racks, referencing new tables that 
    specify the reactivity effects of fuel assembly burnup and decay time, 
    and increasing the listed capacity of the spent fuel pool. These 
    changes would allow the use of credit for soluble boron in the spent 
    fuel criticality analyses. This would allow Florida Power & Light to 
    increase the capacity of the spent fuel storage pool. The proposed 
    action is in accordance with the licensee's application for amendment 
    dated December 31, 1997, as supplemented May 15, September 15, November 
    25, 1998, and January 28, 1999.
    
    The Need for the Proposed Action
    
        The proposed action would increase the allowed storage capacity of 
    the St. Lucie Plant, Unit 2, spent fuel pool (SFP) to 1360 fuel 
    assemblies, allowing the licensee to continue to operate beyond 2001. 
    The Unit 2 SFP at St. Lucie Plant contains 1584 spent fuel storage 
    cells, of which 1076 are currently allowed for storage by the technical 
    specifications. The licensee estimates that, by the year 2001, St. 
    Lucie Plant, Unit 2, will have filled all SFP storage locations not 
    reserved for a full-core off-load of fuel. The projected loss of 
    capability to store spent fuel from future operation of St. Lucie 
    Plant, Unit 2, would affect the licensee's ability to operate St. Lucie 
    Plant, Unit 2. The proposed amendment is needed in order to ensure the 
    capability to perform a full-core off-load to the SFP until 
    approximately 2007.
    
    Environmental Impacts of the Proposed Action
    
    Thermal Impact
        The licensee's thermal analysis on the effects of the proposed 
    change revealed that the proposed increase in storage capacity will 
    change the maximum decay heat load for a partial core offload from 
    16.9E6 Btu/hr to 19.76E6 Btu/hr and for full core offload conditions 
    from 31.7E6 Btu/hr to 35.22E6 Btu/hr. This increased heat load results 
    in an increase of approximately 3 deg.F in the maximum fuel pool water 
    temperature for the partial core offload case, and an increase of 
    approximately 5 deg.F in water temperature for storage of the limiting 
    full core offload (note: maximum fuel pool temperature will be 
    maintained less than or equal to 150 deg.F). The total heat load 
    rejected to the environment by St. Lucie Plant, Unit 2, is about 6.2E9 
    Btu/hr. The percentage increase in the heat rejected to the environment 
    due to the increase in spent fuel storage capacity is on the order of 
    0.05% for partial core discharges and 0.06% for fuel storage following 
    a full core offload. This heat rejection to the environment is not 
    considered a significant increase from current heat rejection levels.
    Radiological Evaluation
        Solid Radioactive Waste. The net effect of increasing the St. 
    Lucie, Unit 2, spent fuel pool storage capacity is that
    
    [[Page 23134]]
    
    older fuel elements will be retained in wet storage beyond the time 
    when they would have otherwise been loaded into casks for dry storage 
    on-site. Retaining already-aged fuel in wet storage for an additional 
    period of time will not appreciably increase the activity in the fuel 
    pool water or the amount of solid radioactive waste which must be 
    disposed of because the short-lived isotopes associated with these fuel 
    bundles will have had an opportunity to decay. Therefore, increasing 
    the fuel pool storage capacity as proposed for St. Lucie, Unit 2, will 
    have no significant effect on the quantity of radioactive waste 
    collected.
        Gaseous Radioactive Waste. Storage of additional quantities of 
    spent fuel in the SFP will not significantly increase the release of 
    gaseous fission products such as Krypton-85 and Iodine-131. Experience 
    has demonstrated that during the period between refueling outages, 
    there is no longer a significant release of fission products, including 
    Krypton-85, from stored spent fuel containing cladding defects. Iodine-
    131 released from spent fuel assemblies to the SFP water will not be 
    significantly increased as a result of the expansion of the fuel 
    storage capacity since the Iodine-131 inventory in the fuel will decay 
    to negligible levels in the period between refueling outages. The 
    licensee has stated that fuel rod integrity at St. Lucie, Unit 2, has 
    been very good, with most fuel cycles evidencing no leaking fuel rods. 
    Additionally, the rod pressure, which tends to act as driving force for 
    fission product release, is substantially decreased after long periods 
    of fuel cooling.
        The increased heat load on the SFP from the storage of additional 
    spent fuel assemblies could potentially result in an increase in the 
    SFP evaporation rate, which may result in a slight increase in the 
    amount of gaseous tritium released from the pool. However, the overall 
    release of radioactive gases from St. Lucie Plant, Unit 2, will remain 
    a small fraction of the limits of 10 CFR Part 20, and is therefore 
    considered insignificant.
        Radioactive Releases Due to Accidents. The existing analyses of 
    record pertaining to the radiological consequences of a fuel handling 
    accident within the St. Lucie Plant, Unit 2, Fuel Handling Building 
    (FHB) and the postulated drop of a spent fuel cask just outside the FHB 
    have been examined to assess the impact of the proposed license 
    amendment. The assumptions and parameters previously employed in 
    evaluating the fuel mishandling accident were consistent with NRC 
    Regulatory Guides 1.13 and 1.25. The previously analyzed consequences 
    of dropping a spent fuel cask were based on the guidelines provided in 
    Section 15.7.5 of the Standard Review Plan. The licensee's review of 
    the existing analysis of the fuel handling accident has concluded that 
    the gap activities provided in the analysis of record for the fuel 
    handling accident conservatively bound those values expected to occur 
    at assembly discharge burnups of up to 60,000 MWD/MTU. As defined by 
    Section 15.7.4 of the Standard Review Plan, calculated dose values are 
    well within the guidelines if the calculated whole body dose is less 
    than or equal to 6 rem and the calculated thyroid dose is less than or 
    equal to 75 rem.
        The proposed license amendment does not involve any changes to the 
    method of operating or range of motion of the spent fuel cask handling 
    crane. No movement of loads in excess of the nominal weight of a fuel 
    assembly, control element assembly, and associated handling tool is 
    permitted over other fuel assemblies in the storage pool. Protection 
    against dropping the spent fuel cask into the spent fuel storage pool 
    is provided by the basic layout of the FHB. As noted in updated final 
    safety analysis report, Section 9.1.4.3.2, additional protection is 
    afforded by the trolley bumpers and a set of limit switches that work 
    together with bridge and trolley brakes to prevent movement of the 
    crane hook into the restricted area.
        The proposed amendment will not involve any changes in the 
    operation or range of motion of the spent fuel handling machine. During 
    movement of a fuel assembly, the load on the hoist cable is monitored 
    to ensure that movement is not restricted. Installed interlocks will 
    continue to restrict movement of the handling machine when the hoist is 
    withdrawing or inserting an assembly.
        The licensee has also examined the existing analysis of an accident 
    involving the drop of a spent fuel cask containing ten irradiated fuel 
    assemblies. This review has determined that conservative input 
    assumptions were used and that the results of the existing analysis are 
    well within the acceptance criteria for a Limiting Fault-2 event.
        Increasing the storage capacity of the St. Lucie, Unit 2, SFP as 
    described in this proposed license amendment will have no effect on the 
    radiological consequences of an assumed fuel mishandling event or on 
    the consequences of dropping a loaded spent fuel cask. For each of 
    these events, the calculated doses are small relative to the guideline 
    values.
        The impact of the proposed increase in St. Lucie, Unit 2, spent 
    fuel storage capacity and the implications of the use of reactivity 
    credit for fuel pool soluble boron have been examined in the above 
    discussion. Each of the impacts of the proposed change has been 
    quantified and determined to be within acceptable limits by comparison 
    to established acceptance criteria.
        Accordingly, the Commission concludes that there are no significant 
    environmental impacts associated with the proposed action.
    
    Summary
    
        The Commission has completed its evaluation of the proposed action. 
    The proposed action will not increase the probability or consequences 
    of accidents, no changes will be made in the types of any effluents 
    that may be released off-site, and there will be no significant 
    increase in occupational or public radiation exposure. Accordingly, the 
    Commission concludes that there are no significant radiological 
    environmental impacts associated with the proposed action.
        With regard to potential non-radiological impacts, the proposed 
    action involves features located entirely within the restricted area as 
    defined in 10 CFR Part 20. It will not affect non-radiological plant 
    effluents and has no other environmental impact. The proposed action 
    does not involve any historic sites. Therefore, there are no 
    significant non-radiological environmental impacts associated with the 
    proposed action. Accordingly, the Commission concludes that there are 
    no significant environmental impacts associated with the proposed 
    action.
    
    Alternatives to the Proposed action
    
    Shipping Fuel to a Permanent Federal Fuel Storage/Disposal Facility
        Shipment of spent fuel to a high-level radioactive storage facility 
    is an alternative to increasing the onsite spent fuel storage capacity. 
    However, the U.S. Department of Energy's (DOE's) high-level radioactive 
    waste repository is not expected to begin receiving spent fuel until 
    approximately 2010 at the earliest. In October 1996, the Administration 
    did commit DOE to begin storing waste at a centralized location by 
    January 31, 1998. However, no location has been identified and an 
    interim federal storage facility has yet to be identified in advance of 
    a decision on a permanent repository. Therefore, shipping spent fuel to 
    the DOE repository is not considered an alternative to increased
    
    [[Page 23135]]
    
    onsite spent fuel storage capacity at this time.
    Shipping Fuel to a Reprocessing Facility
        Reprocessing of spent fuel from the St. Lucie Plant, Unit 2, is not 
    a viable alternative since there are no operating commercial 
    reprocessing facilities in the United States. Spent fuel would have to 
    be shipped to an overseas facility for reprocessing. This approach has 
    never been used and it would require approval by the U.S. Department of 
    State as well as other entities. Additionally, the cost of spent fuel 
    reprocessing is not offset by the salvage value of the residual uranium 
    and reprocessing represents an added cost. Therefore, this alternative 
    is considered unacceptable.
    Shipping Fuel to Another Utility or Site or to St. Lucie, Unit 1, for 
    Storage
        Shipment of irradiated fuel from St. Lucie, Unit 2, to Turkey Point 
    or to the St. Lucie, Unit 1, fuel pool would provide short-term relief 
    from the storage problem at St. Lucie, Unit 2, but this transfer of 
    fuel between units would create no additional storage locations for 
    irradiated fuel. As a result, any fuel transfer would accelerate the 
    loss of fuel pool storage at the receiving unit and give no benefit to 
    the facility. Currently, the Turkey Point site has installed fuel pool 
    storage capacity sufficient to handle site requirements for irradiated 
    fuel storage until approximately the end of licensed life in 2012 (for 
    Unit 3) and 2013 (for Unit 4). Further expansion of the storage 
    capacity of the Turkey Point spent fuel pools is not feasible. Unlike 
    the situation at Turkey Point, the St. Lucie site will require 
    development of an Independent Spent Fuel Storage Facility (ISFSI) to 
    permit operation to the end of licensed life. As a result, shipment of 
    irradiated fuel from St. Lucie to Turkey Point would require the early 
    development of an ISFSI at Turkey Point without eliminating the 
    requirement to subsequently develop an ISFSI at the St. Lucie site. 
    Additionally, the design of the Turkey Point fuel pool storage racks 
    has been optimized for storage of fuel with a different lattice and 
    different reactivity characteristics than that used at St. Lucie, Unit 
    2; thus, storage of Unit 2 fuel at Turkey Point would both limit 
    storage of future discharged Turkey Point fuel and represent a less 
    than optimal use of the existing Turkey Point storage capability.
        Likewise, the shipment of irradiated fuel from St. Lucie, Unit 2, 
    to St. Lucie, Unit 1, for storage does not eliminate the need to 
    develop additional spent fuel storage capability at the St. Lucie site 
    in the future. FPL knows of no other utility that is prepared to accept 
    shipments of irradiated fuel from St. Lucie, Unit 2, for long-term 
    storage at its site.
        For these reasons, and considering the increased fuel handling and 
    additional occupational radiation exposure incurred during the shipment 
    of irradiated fuel, the alternative of shipping St. Lucie, Unit 2, fuel 
    to Turkey Point or to St. Lucie, Unit 1, for storage is not an 
    acceptable alternative to the proposed action.
    Alternatives Creating Additional Storage Capacity
        A variety of alternatives to increase the storage capacity of the 
    St. Lucie, Unit 2, spent fuel pool were considered prior to developing 
    the proposed license amendment based on soluble boron credit. Fuel rod 
    consolidation was examined as a potential alternative and was 
    eliminated because of the limited industry experience in disassembling 
    irradiated fuel and because of the potential for fission product 
    release due to rod breakage during disassembly. Additionally, because 
    the Department of Energy (DOE) considers consolidated fuel to be a non-
    standard waste form, FPL was concerned that the presence of fuel in 
    this form would cause the DOE to delay its acceptance of waste from St. 
    Lucie, Unit 2.
        The addition of poison inserts to the Unit 2 fuel pool was examined 
    and later rejected because the large quantity of inserts necessary to 
    adequately control the fuel pool reactivity had a significantly greater 
    initial cost that the alternative selected. Additionally, use of poison 
    inserts increases the volume of radioactive waste that must be disposed 
    of or decontaminated during decommissioning of the spent fuel pool, 
    making this alternative unacceptable.
        The early implementation of dry cask storage for irradiated fuel at 
    the St. Lucie site was also considered. Dry cask storage involves 
    transferring irradiated fuel, after several years of storage in the 
    Unit 2 fuel pool, to high capacity casks with passive heat dissipation 
    features. After loading, these casks would be placed on a concrete pad 
    at an outdoor location on the St. Lucie site. This alternative was 
    rejected by FPL because each of the alternatives discussed above would 
    provide additional storage locations for irradiated fuel at lower cost 
    and with less environmental impact.
        As a result, FPL concluded that none of the alternative 
    technologies that could create additional spent fuel storage capacity 
    at St. Lucie, Unit 2, could do so with an environmental impact less 
    than the impacts associated with the chosen option.
    Reduction of Spent Fuel Generation
        To minimize the quantities of irradiated fuel generated during full 
    power operation at St. Lucie, FPL has developed efficient fuel loading 
    patterns that maximize the utilization of fissile material within each 
    assembly consistent with license limits on the integrated fuel rod 
    exposure. Batch discharge burnups for St. Lucie, Unit 2, fuel regularly 
    approximate 45 GWD/MTU with peak assembly burnups reaching 50 GWD/MTU 
    by the time of discharge. St. Lucie, Unit 2, consistently depletes fuel 
    assemblies to these burnups without experiencing cladding perforations 
    so that the fission product inventory present in the spent fuel pool 
    water remains low. The high values of batch average and peak assembly 
    discharge burnup ensure that the electricity generated by St. Lucie, 
    Unit 2, yields the minimum possible amount of spent fuel.
        The fuel assembly design used at St. Lucie, Unit 1, and at Turkey 
    Point is not compatible with the St. Lucie, Unit 2, core. As a result, 
    partially irradiated fuel from other FPL nuclear units can not be used 
    at Unit 2 (or vice versa) to reduce the rate of spent fuel discharge.
        Operation of St. Lucie, Unit 2, at a reduced power level for long 
    periods of time would extend the existing spent fuel pool storage 
    capacity. However, to compensate for the reduced generation by St. 
    Lucie, Unit 2, another power generation facility would be required to 
    increase its power output, possibly resulting in an increase in 
    airborne pollution and greenhouse gas emissions. The adverse 
    environmental impact of increased airborne pollution and greenhouse gas 
    emissions resulting from a long-term derate of St. Lucie, Unit 2, 
    generating capacity is significantly greater than the environmental 
    impact associated with increasing the storage capacity of the existing 
    Unit 2 spent fuel pool.
    
    The No-Action Alternative
    
        As an alternative to the proposed action, the NRC staff considered 
    denial of the proposed action (i.e., the ``no-action'' alternative). 
    Denial of the application would result in no significant change in 
    current environmental impacts. The environmental impacts of the 
    proposed action and the alternative action are similar.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the Final Environmental Statement for St. 
    Lucie, Unit 2.
    
    [[Page 23136]]
    
    Agencies and Persons Consulted
    
        By Letter dated March 8, 1991, Mary E. Clark of the State of 
    Florida, Department of Health and Rehabilitative Services, informed 
    Deborah A. Miller, Licensing Assistant, U.S. NRC, that the State of 
    Florida does not desire notification of issuance of license amendments. 
    Thus, the State official had no comments.
    
    Finding of No Significant Impact
    
        On the basis of the environmental assessment, the Commission 
    concludes that the proposed action will not have a significant effect 
    on the quality of the human environment. Accordingly, the Commission 
    has determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated December 31, 1997, as supplemented May 15, 
    1998, September 15, 1998, November 25, 1998, and January 28, 1999. The 
    May 15, 1998 supplement was a result of an U.S. Nuclear Regulatory 
    Commission request for additional information dated April 8, 1998. All 
    of these documents are available for public inspection at the 
    Commission's Public Document Room, The Gelman Building, 2120 L Street, 
    NW., Washington, DC, and at the local public document room located at 
    the Indian River Community College Library, 3209 Virginia Avenue, Fort 
    Pierce, Florida 34981-5596.
    
        Dated at Rockville, Maryland, this 23rd day of April 1999.
    
        For the Nuclear Regulatory Commission.
    William C. Gleaves,
    Project Manager, Section 2, Project Directorate II, Division of 
    Licensing Project Management, Office of Nuclear Reactor Regulation.
    [FR Doc. 99-10685 Filed 4-28-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
04/29/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-10685
Pages:
23133-23136 (4 pages)
Docket Numbers:
Docket No. 50-389
PDF File:
99-10685.pdf