99-8503. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 66 (Wednesday, April 7, 1999)]
    [Notices]
    [Pages 17021-17040]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-8503]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Pub. L. 97-415, the U.S. Nuclear Regulatory Commission 
    (the Commission or NRC staff) is publishing this regular biweekly 
    notice. Pub. L. 97-
    
    [[Page 17022]]
    
    415 revised section 189 of the Atomic Energy Act of 1954, as amended 
    (the Act), to require the Commission to publish notice of any 
    amendments issued, or proposed to be issued, under a new provision of 
    section 189 of the Act. This provision grants the Commission the 
    authority to issue and make immediately effective any amendment to an 
    operating license upon a determination by the Commission that such 
    amendment involves no significant hazards consideration, 
    notwithstanding the pendency before the Commission of a request for a 
    hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 13, 1999, through March 26, 1999. The 
    last biweekly notice was published on March 24, 1999 (64 FR 14278).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By April 23, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The
    
    [[Page 17023]]
    
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: February 26, 1999.
        Description of amendments request: The proposed amendment would 
    revise Technical Specification (TS) 3.5.3, ``Emergency Core Cooling 
    System--Operating,'' to extend the completion time for one inoperable 
    low pressure safety injection subsystem from 72 hours to 7 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The proposed amendment will extend the Completion Time 
    for one inoperable low pressure safety injection (LPSI) subsystem in 
    Technical Specification (TS) 3.5.3, Emergency Core Cooling Systems 
    (ECCE)[S]--Operating, from 72 hours to 7 days. The LPSI subsystem is 
    part of the ECCS train and part of the shutdown cooling subsystem. 
    The LPSI components are not accident initiators in any accident 
    previously evaluated. Therefore, this change does not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The LPSI system is primarily designed to mitigate the 
    consequences of a large break loss of coolant accident (LOCA). These 
    proposed changes do not affect any of the assumptions used in the 
    deterministic LOCA analysis.
        In order to evaluate the LPSI Completion Time extension with 
    respect to the ECCS, probabilistic safety analysis (PSA) methods 
    were utilized. The results of these analyses show no significant 
    increase in the core damage frequency. As a result, there would be 
    no significant increase in the consequences of an accident 
    previously evaluated. These analyses are detailed in CE NPSD-995, 
    Combustion Engineering Owners Group ``Joint Applications Report for 
    Low Pressure Safety Injection System AOT Extension,'' May 1995, as 
    supplemented by updated PVNGS data provided in the attachment to 
    this enclosure.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The proposed amendment will extend the Completion Time for one 
    inoperable low pressure safety injection (LPSI) subsystem in 
    Technical Specification (TS) 3.5.3, Emergency Core Cooling Systems 
    (ECCE)[S]--Operating, from 72 hours to 7 days. The proposed change 
    does not change the design, configuration, or method of operation of 
    the plant. Therefore, this change does not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not involve a significant reduction in 
    a margin of safety. The proposed amendment will extend the 
    Completion Time for one inoperable low pressure safety injection 
    (LPSI) subsystem in Technical Specification (TS) 3.5.3, Emergency 
    Core Cooling Systems (ECCE)[S]--Operating, from 72 hours to 7 days. 
    The proposed change does not affect the limiting conditions for 
    operation or their bases used in the deterministic analyses to 
    establish the margin of safety. PSA evaluations were used to 
    evaluate these changes. These evaluations demonstrate that the 
    changes will be risk neutral or risk beneficial for PVNGS. These 
    evaluations are detailed in CE NPSD-995, as supplemented by updated 
    data provided in the attachment to this enclosure.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999.
        NRC Project Director: William H. Bateman.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: January 22, 1999.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TSs) Sections 3.7.D.1.g, 6.2.2.h and 
    6.3.1. Specifically, (1) Section 3.7.D.1.g would be revised to correct 
    an editorial error; (2) Section 6.2.2.h would be revised to change the 
    senior reactor operator license requirement for the Operations Manager; 
    and (3) Section 6.3.1 would modify the qualification requirement for 
    the Operations Manager.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change [to Section 3.7.D.1.g] is administrative in 
    nature. It involves making an editorial change to provide the 
    correct functional description of the breakers. This change does not 
    affect possible initiating events for accidents previously evaluated 
    or alter the configurations or operation of the facility. The 
    Limiting Safety Systems Settings and Safety Limits specified in the 
    current Technical Specifications
    
    [[Page 17024]]
    
    remain unchanged. Therefore, the proposed change to the subject 
    Technical Specification would not increase the probability or 
    consequences of an accident previously evaluated.
        The proposed change [to Section 6.2.2.h] is administrative in 
    nature. The individual who provides the day to day direction of the 
    activities of the operating shift will still possess an SRO [Senior 
    Reactor Operator] license and this proposed change is consistent 
    with the statement in NUREG-1431, Section 5.2.2.f. This change does 
    not affect possible initiating events for accidents previously 
    evaluated or alter the configuration or operation of the facility. 
    The Limiting Safety Systems Settings and Safety Limits specified in 
    the current Technical Specifications remain unchanged. Therefore, 
    the proposed change to the subject Technical Specification would not 
    increase the probability or consequences of an accident previously 
    evaluated.
        The proposed change [to Section 6.3.1] is administrative in 
    nature. The individual who provides the day to day direction of the 
    activities of the operating shift will still possess an SRO license 
    and this proposed change is consistent with the statement in NUREG-
    1431, Section 5.2.2.f. This change does not affect possible 
    initiating events for accidents previously evaluated or alter the 
    configuration or operation of the facility. The Limiting Safety 
    Systems Settings and Safety Limits specified in the current 
    Technical Specifications remain unchanged. Therefore, the proposed 
    change to the subject Technical Specification would not increase the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        As stated above, the proposed change [to Section 3.7.D.1.g] is 
    administrative in nature. The safety analysis of the facility 
    remains complete and accurate. There are no physical changes to the 
    facility and the plant conditions for which the design basis 
    accidents have been evaluated are still valid. The operating 
    procedures and emergency procedures are unaffected. Consequently, no 
    new failure modes are introduced as a result of the proposed change. 
    Therefore, the proposed change will not initiate any new or 
    different kind of accident.
        The proposed change [to Section 6.2.2.h] is administrative in 
    nature. The safety analysis of the facility remains complete and 
    accurate. There are no physical changes to the facility and the 
    plant conditions for which the design basis accidents have been 
    evaluated are still valid. The operating procedures and emergency 
    procedures are unaffected. Consequently, no new failure modes are 
    introduced as a result of the proposed changes. Therefore, the 
    proposed change will not initiate any new or different kind of 
    accident.
        The proposed change [to Section 6.3.1] is administrative in 
    nature. The safety analysis of the facility remains complete and 
    accurate. There are no physical changes to the facility and the 
    plant conditions for which the design basis accidents have been 
    evaluated are still valid. The operating procedures and emergency 
    procedures are unaffected. Consequently, no new failure modes are 
    introduced as a result of the proposed changes. Therefore, the 
    proposed change will not initiate any new or different kind of 
    accident.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change [to Section 3.7.D.1.g] is administrative in 
    nature. Since there are no changes to the operation of the facility 
    or physical design the Updated Final Safety Analysis Report (UFSAR) 
    design basis, accident assumptions, or Technical Specification Bases 
    are not affected. Therefore, the proposed changes will not result in 
    a reduction in the margin of safety.
        The proposed change [to Section 6.2.2.h] is administrative in 
    nature. Since there are no changes to the operation of the facility 
    or physical design the Updated Final Safety Analysis Report (UFSAR) 
    design basis, accident assumptions, or Technical Specification Bases 
    are not affected. Therefore, the proposed changes will not result in 
    a reduction in the margin of safety.
        The proposed change [to Section 6.3.1] is administrative in 
    nature. Since there are no changes to the operation of the facility 
    or physical design the Updated Final Safety Analysis Report (UFSAR) 
    design basis, accident assumptions, or Technical Specification Bases 
    are not affected. Therefore, the proposed changes will not result in 
    a reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: January 22, 1999.
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications (TSs) Section 4.3. Specifically, the 
    revision would permit the reactor coolant system (RCS) leak test to be 
    performed at normal operating pressure after it has been closed 
    following normal opening in lieu of a hydrostatic test being performed 
    at 2335 psig.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The change proposes a system leakage test for 
    the RCS that is comparable to the hydrostatic test that it replaces, 
    as acknowledged by the NRC approval of ASME Code Case N-498, 
    ``Alternative Rules for 10-Year Hydrostatic Pressure Testing for 
    Class 1 and 2 Systems Section XI, Division 1,'' and the ASME 
    [American Society for Mechanical Engineers] Boiler and Pressure 
    Vessel Code, Section XI. [. . .] The proposed change to substitute a 
    system leak test at normal operating pressure in lieu of the 
    hydrostatic test at 2335 psig will minimize challenge to plant 
    safety and demonstrate leak tightness of the RCS. Therefore, the 
    proposed change would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed license amendment does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated. The proposed changes do not involve the addition of any 
    new or different type of equipment, nor do they involve the 
    operation of equipment required for safe operation of the facility 
    in a manner different from those addressed in the Updated Final 
    Safety Analysis Report. [. . .] Based on industry experience, it is 
    expected that any leaks would be discovered by the leak test at 
    normal operating pressure.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed license amendment does not involve a significant 
    reduction in a margin of safety. The proposed changes do not 
    adversely affect performance of any safety related system or 
    component, instrument operation, or safety system setpoints and do 
    not result in increased severity of any of the accidents considered 
    in the safety analysis. Although the current basis states that if 
    the system does not leak at 2335 psig (operating pressure + 100 
    psig) it will be leak tight during normal operation, industry 
    experience demonstrates that leaks are not discovered as a result of 
    hydrostatic test pressure propagating a preexisting flaw through 
    wall. In most cases, leaks are discovered when the system is at 
    normal operating pressure. Also, testing will continue to be 
    performed as required by the ASME Boiler and Pressure Vessel Code 
    Section XI.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.
    
    [[Page 17025]]
    
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: S. Singh Bajwa, Director.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: March 8, 1999.
        Description of amendment request: The proposed amendments would 
    delete certain requirements from Technical Specification (TS) Section 
    6.0 ``Administrative Controls'' that are adequately controlled by 
    existing regulations, other than 10 CFR 50.36 and the TS. The 
    amendments also relocate selected requirements from TS Section 6.0 to 
    the licensee's controlled documents such as the Turkey Point Units 3 
    and 4 Updated Final Safety Analysis Report (UFSAR). The amendments also 
    clarify certain provisions of TS Section 6.0. The proposed changes are 
    to relocate, revise, delete, or clarify the following provisions of the 
    TS:
    
    ------------------------------------------------------------------------
      Existing TS section            Subject              Proposed change
    ------------------------------------------------------------------------
    6.2.2.f................  Administrative Controls  Partly delete, partly
                              on Working Hours of      relocate within TS.
                              Plant Staff.
    Table 6.2-1............  Minimum Shift Crew       Clarify.
                              Composition.
    6.2.3..................  Shift Technical Advisor  Clarify.
    6.4....................  Training...............  Delete.
    6.5....................  Review and Audit.......  Relocate to UFSAR.
    6.6....................  Reportable Event Action  Partly delete, partly
                                                       relocate to UFSAR.
    6.8.2..................  Review and Approval of   Relocate to UFSAR.
                              Procedures.
    6.8.3..................  Temporary Changes to     Relocate to UFSAR.
                              Procedures.
    6.8.4.b................  In-Plant Radiation       Relocate to UFSAR.
                              Monitoring.
    6.8.4.g................  Radiological             Relocate to UFSAR.
                              Environmental
                              Monitoring Program.
    6.10...................  Record Retention.......  Relocate to UFSAR.
    6.11...................  Radiation Protection     Relocate to UFSAR.
                              Program.
    6.12...................  High Radiation Area....  Clarify.
    6.13...................  Process Control Program  Relocate to UFSAR.
                              (PCP).
    6.14...................  Offsite Dose             Revise to reflect
                              Calculation Manual       changes to 6.5 &
                              (ODCM).                  6.10.
    ------------------------------------------------------------------------
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of the plant in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed changes are administrative in nature. These 
    proposed changes will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated 
    because they do not affect assumptions contained in plant safety 
    analyses, the physical design and/or operation of the plant, nor do 
    they affect Technical Specifications that preserve safety analysis 
    assumptions. None of the proposed changes involve a physical 
    modification to the plant, a new mode of operation or a change to 
    the UFSAR transient analyses. No Limiting Condition for Operation, 
    ACTION statement or Surveillance Requirement is affected by any of 
    the proposed changes. Also, these proposed changes, in themselves, 
    do not reduce the level of qualification or training such that 
    personnel requirements would be decreased. Further, the Proposed 
    changes do not alter the design, function, or operation of any plant 
    component. Therefore, the proposed changes do not affect the 
    probability or consequences of accidents previously evaluated.
        2. Operation of the plant in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    The changes being proposed are administrative in nature and do not 
    affect assumptions contained in plant safety analyses, the physical 
    design and/or modes of plant operation defined in the plant 
    operating license, or Technical Specifications that preserve safety 
    analysis assumptions. The proposed changes do not introduce a new 
    mode of plant operation or surveillance requirement, nor involve a 
    physical modification to the plant. The proposed changes are 
    administrative in nature. The changes propose to revise, delete, or 
    relocate the stated administrative control provisions from the TS to 
    the UFSAR whereby adequate control of information is maintained. 
    Furthermore, the proposed changes do not alter the design, function, 
    or operation of any plant components. Therefore, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Operation of the plant in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The proposed changes do not involve a significant reduction in a 
    margin of safety because they are administrative in nature. The 
    operating limits and functional capabilities of the affected 
    systems, structures, and components are unchanged by the proposed 
    amendments. None of the proposed changes involve a physical 
    modification to the plant, a new mode of operation or a change to 
    the UFSAR transient analyses. No Limiting Condition for Operation, 
    ACTION statement, or Surveillance Requirement is affected. 
    Additionally, the proposed changes do not alter the scope of 
    equipment currently required to be OPERABLE or subject to 
    surveillance testing, nor does the proposed change affect any 
    instrument setpoints or equipment safety functions. Therefore, the 
    change does not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
        Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420.
        NRC Project Director: Cecil O. Thomas.
    
    [[Page 17026]]
    
    GPU Nuclear, Inc. etal., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey
    
        Date of amendment request: December 23, 1998.
        Description of amendment request: The proposed Technical 
    Specification (TS) change request will change the surveillance 
    frequency for verifying the operability of motor-operated isolation 
    valves and condensate makeup valves in the Isolation Condenser TS 
    4.8.A.1 and Bases page from once per month to once per 3 months.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed TS change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed surveillance interval change does not alter the 
    actual surveillance requirements, nor does it alter the limits and 
    restrictions on plant operations. The reliability of systems and 
    components relied upon to prevent or mitigate the consequences of 
    accidents previously evaluated is not degraded by the proposed 
    change to the surveillance interval. Assurance of system and 
    equipment availability is maintained. The proposed change does not 
    alter any system or equipment configuration.
        Based on the above, the proposed change does not significantly 
    increase the probability or consequences of a[n] accident previously 
    evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed surveillance interval change does not alter the 
    actual surveillance requirements, nor does it alter the limits and 
    restrictions on plant operations. Assurance of system and equipment 
    availability is maintained. The proposed change does not alter any 
    system or equipment configuration nor does it introduce any new 
    mechanisms which could contribute to the creation of a new or 
    different kind of accident than previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The proposed change extends the surveillance interval for 
    verifying the operability of Isolation Condenser motor-operated 
    isolation valves and condensate makeup valves from once per month to 
    once per three months. The proposed change does not alter the actual 
    surveillance requirements, the limits and restrictions on plant 
    operations nor the design, function or manner of operation of any 
    structures, systems or components. System availability and 
    reliability are maintained. Accordingly, the proposed TS change does 
    not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Elinor G. Adensam.
    
    GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey
    
        Date of amendment request: February 12, 1999.
        Description of amendment request: The proposed Technical 
    Specification (TS) change will delete the organizational chart and the 
    related organizational references from the Appendix B Environmental TS 
    and revise the appearance and format of the Environmental TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because deletion of the organization charts and other 
    organizational references in the [Environmental Technical 
    Specifications] ETS does not affect plant operation. GPU Nuclear 
    will continue to inform the NRC of organizational changes through 
    other required controls.
        2. The proposed change does not create the possibility of a new 
    or different type of accident than previously evaluated because the 
    proposed change is administrative in nature, and no physical 
    alteration of plant configuration, changes to setpoints or operating 
    parameters are proposed.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety because it does not alter the design, 
    function or manner of operation of any structures, systems or 
    components. Organizational structure or its representation does not 
    directly impact the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Elinor G. Adensam.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa.
    
        Date of amendment request: February 18, 1999.
        Description of amendment request: The proposed amendment would 
    revise Duane Arnold Energy Center (DAEC) Technical Specification (TS) 
    Table 3.3.6.1-1, ``Primary Containment Isolation Instrumentation,'' by 
    deleting the manual initiation function of the high pressure coolant 
    injection (HPCI) system and reactor core isolation cooling (RCIC) 
    system isolation. A related condition as well as corresponding 
    surveillance requirements and bases would also be deleted. Thus, the 
    change would (1) revise Table 3.3.6.1-1 by removing items 3j. and 4.j.; 
    (2) revise Note 2 to Surveillances to Licensing Condition for Operation 
    (LCO) 3.3.6.1 by deleting information regarding items 3 j. and 4.j.; 
    and (3) revise LCO 3.3.6.1 by removing Condition G and Surveillance 
    Requirement 3.3.6.1.10.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        After reviewing this proposed amendment, we [the licensee] have 
    concluded:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. The Manual Initiation Function for HPCI and 
    RCIC Isolation is not considered to be an initiator for any accident 
    previously evaluated in the UFSAR. Therefore, this change does not 
    involve a significant increase in the probability of any previously 
    evaluated accidents. The Manual Initiation push button channels 
    introduce signals into HPCI and RCIC System isolation logics that 
    are redundant to the automatic protective instrumentation and 
    provide manual isolation capability only if a system initiation 
    signal is present. Technical Specification Section 3.3.6.1 Condition 
    G requires isolation of the System flowpath, which renders the 
    System inoperable and reduces the availability of the System due to 
    the failure of a manually initiated isolation, an isolation which is 
    not assumed in any transient or accident analysis in the UFSAR. 
    Removal of the Manual Initiation Function
    
    [[Page 17027]]
    
    for HPCI and RCIC from the Primary Containment Isolation 
    Instrumentation Section of Technical Specifications does not affect 
    the automatic protective instrumentation and the automatic isolation 
    capability. Therefore, this change does not significantly increase 
    the consequences of a previously analyzed accident.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The proposed change introduces no new mode of plant 
    operation and does not involve physical modification to the plant. 
    Therefore, it does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed amendment will not involve a significant 
    reduction in a margin of safety. The proposed change deletes the 
    Manual Initiation Function from Technical Specifications, but no 
    significant reduction in a margin of safety is involved. Technical 
    Specification Section 3.3.6.1 Condition G requires isolation of the 
    System flowpath, which renders the System inoperable and reduces the 
    availability of the System due to the failure of a manually 
    initiated isolation, an isolation that is not assumed in any 
    transient or accident analysis in the UFSAR. Removal of the Manual 
    Initiation Function for HPCI and RCIC from the Primary Containment 
    Isolation Instrumentation Section of Technical Specifications does 
    not affect the automatic protective instrumentation and the 
    isolation capability. This change is acceptable based on the fact 
    that the Manual Initiation Function is not assumed in any accident 
    or transient analysis in the UFSAR.
        Based upon the above, we [licensee] have determined that the 
    proposed amendment will not involve a significant hazards 
    consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, IA 52401.
        Attorney for licensee: Jack Newman, Al Gutterman, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: T.J. Kim, Acting.
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: March 1, 1999.
        Description of amendment request: The proposed amendment would 
    change the Cooper Nuclear Station (CNS) Technical Specifications (TSs) 
    to revise the calibration frequency of the reactor recirculation flow 
    transmitters from once every 184 days to once every 18 months. This 
    calibration is required as part of TS Surveillance Requirement (SR) 
    3.3.1.1.10.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Changing the calibration frequency of the recirculation 
    loop flow transmitters from 184 days to 18 months may increase the 
    amount of drift experienced by the transmitters. However, CNS 
    calculation (NEDC 98-024 [forwarded by letter dated March 10, 1999]) 
    takes into account the 18 month calibration intervals. This 
    calculation, performed in accordance with the General Electric (GE) 
    setpoint methodology for CNS, demonstrates that the expected drift 
    is not significant, and is consistent with past operating 
    experience. Changing the calibration frequency of the flow 
    transmitters does not change any of the precursors assumed in the 
    accident analysis. Therefore, changing the calibration frequency for 
    flow transmitters from 184 days to 18 months does not involve a 
    significant increase in the probability of an accident previously 
    evaluated in the USAR [Updated Safety Analysis Report].
        The proposed change will not create the possibility of a new or 
    different kind of accident than evaluated in the USAR. The proposed 
    change does not result in any physical change to plant structures, 
    systems, or components. The proposed change does not alter the form, 
    fit, or function of any equipment or components credited in the 
    accident analyses described in the USAR. Therefore, changing the 
    test frequency does not create the possibility of a new or different 
    kind of accident.
        The proposed change will not involve a significant reduction in 
    a margin of safety. This conclusion is based on the fact that the 
    proposed change is consistent with the drift assumptions used in CNS 
    approved calculation (NEDC 98-024). The calibration frequency of 18 
    months is consistent with the operating practices prior to 
    conversion to Improved Technical Specifications, and is consistent 
    with past operating practice at CNS. Therefore, changing the 
    calibration frequency from 184 days to 18 months does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Auburn Memorial Library, 1810 
    Courthouse Avenue, Auburn, Nebraska 68305.
        Attorney for licensee: Mr. John R. McPhail, Nebraska Public Power 
    District, Post Office Box 499, Columbus, Nebraska 68602-0499.
        NRC Project Director: George Dick, Acting.
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket Nos. 50-336 
    and 50-423, Millstone Nuclear Power Station, Unit Nos. 2 and 3, New 
    London County, Connecticut
    
        Date of amendment request: March 5, 1999.
        Description of amendment request: The proposed amendment would 
    relocate certain Technical Specification (TS) Section 6.0 
    administrative controls to the NRC-approved Northeast Utilities Quality 
    Assurance Program (NUQAP) Topical Report. Specifically, Sections 6.2.3 
    (Unit 3 only), 6.5, 6.6 (partial), 6.7 (partial), and 6.10. The 
    proposed amendment would also delete parts of Section 6.6 and 6.7 
    because their requirements are duplicated in existing regulations or 
    elsewhere in the TS. In addition, the proposed amendment would modify 
    the table of contents and other TS sections to incorporate the 
    aforementioned changes (e.g., correct references).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        In accordance with 10 CFR 50.92, NNECO has reviewed the attached 
    proposed changes and has concluded that they do not involve a 
    Significant Hazards Consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10 CFR 50.92 are not 
    compromised. The proposed changes are not a SHC because the proposed 
    change will not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        No design basis accidents are affected by these proposed 
    changes. The proposed changes relocate portions of the Technical 
    Specifications to the NUQAP Topical Report or remove duplicate 
    sections and are being proposed to eliminate the need for a T.S. 
    change each time there is a related change in the administrative 
    controls for the site.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        There are no changes in the way the plant is operated due to 
    these revisions. The potential for an unanalyzed accident is not 
    created. There is no impact on plant response, and no new failure 
    modes are introduced. The proposed deletions and
    
    [[Page 17028]]
    
    editorial changes have no impact on safety limits or design basis 
    accidents, and have no potential to create a new or unanalyzed 
    event.
        3. Involve a significant reduction in a margin of safety.
        These changes do not directly affect any protective boundaries 
    nor do they impact the safety limits for the protective boundaries. 
    These proposed changes relocate portions of the administrative 
    controls to the NUQAP Topical Report or are editorial in nature. 
    Therefore, there is no reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    Connecticut.
        NRC Project Director: Elinor G. Adensam.
    
    PECO Energy Company, Docket No. 50-353, Limerick Generating Station, 
    Unit 2, Montgomery County, Pennsylvania
    
        Date of amendment request: March 11, 1999.
        Description of amendment request: The proposed revision to the 
    Technical Specifications (TSs) involves a change to TS Section 2.1 and 
    its associated TS Bases to revise the minimum critical power ratio 
    (MCPR) Safety Limits for Cycle 6.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The revised MCPR Safety Limits for LGS Unit 2 Technical 
    Specifications, and their use to determine cycle-specific thermal 
    limits, have been calculated using NRC-approved methods (i. e, 
    GESTAR-II, Rev. 13) and are based on LGS, Unit 2, Cycle 6 specific 
    inputs. The use of these methods assures that the SLMCPR [safety 
    limit minimum critical power ratio] value is within the existing 
    design and licensing basis, and cannot increase the probability or 
    severity of an accident.
        The basis for the MCPR Safety Limit calculation is to ensure 
    that greater than 99.9 percent of all fuel rods in the core avoid 
    transition boiling if the limit is not violated. The MCPR Safety 
    Limit preserves the existing margin to transition boiling and fuel 
    damage in the event of a postulated accident. The probability of 
    fuel damage is not increased.
        Therefore, the proposed TS changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The MCPR Safety Limit is a Technical Specification numerical 
    value designed to ensure that fuel damage from transition boiling 
    does not occur as a result of the limiting postulated accident. The 
    MCPR Safety Limit is not an accident initiator; therefore, it cannot 
    create the possibility of any new type of accident. The new MCPR 
    Safety Limits are calculated using NRC-approved methods (i.e., 
    GESTAR-II, Rev. 13) and are based on LGS, Unit 2, Cycle 6 specific 
    inputs.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in the margin of safety.
        The margin of safety as defined in the TS Bases will remain the 
    same. The new MCPR Safety Limits are calculated using NRC-approved 
    methods (i.e., GESTAR-II, Rev. 13), which are in accordance with the 
    current fuel design and licensing criteria, and are based on LGS, 
    Unit 2, Cycle 6 specific inputs. The MCPR Safety Limit remains high 
    enough to ensure that greater than 99.9 percent of all fuel rods in 
    the core will avoid transition boiling if the limit is not violated, 
    thereby preserving the fuel cladding integrity.
    
        Therefore, the proposed TS changes do not involve a reduction in 
    the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101.
        NRC Project Director: Elinor G. Adensam.
    
    PP&L, Inc., Docket No. 50-387, Susquehanna Steam Electric Station, Unit 
    1, Luzerne County, Pennsylvania
    
        Date of amendment request: March 12, 1999.
        Description of amendment request: The amendment would modify the 
    Susquehanna Steam Electric Station, Unit 1, Technical Specifications 
    Table 3.3.5.1-1 ``Emergency Core Cooling System Instrumentation.'' The 
    change updates the allowable values for both the Core Spray (CS) and 
    Low Pressure Coolant Injection System (LPCI) ``Reactor Steam Dome 
    Pressure--Low'' functions for initiation and injection permissive. 
    Specifically, the allowable values are being changed from a specified 
    minimum pressure to a specified allowable pressure band. This more 
    restrictive allowable value range will prevent CS and LPCI system 
    overpressurization while still permitting injection to prevent fuel 
    clad temperature limits from being exceeded.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This proposal does not involve an increase in the probability or 
    consequences of an accident previously evaluated. The proposed 
    amendment changes the ``Reactor Steam Dome Pressure-Low'' Allowable 
    Values so to provide further assurance that the Core Spray and RHR 
    systems will perform their LOCA [Loss-of-coolant accident] design 
    basis function.
        The functional design basis of the Core Spray and LPCI is to 
    inject water into the reactor vessel to cool the core during a LOCA 
    by opening the Core Spray and LPCI injection valves when reactor 
    pressure drops below the reactor vessel low pressure permissive. The 
    upper analytical limit for the permissive is the Core Spray and LPCI 
    systems' maximum design pressure, and the lower analytical limit is 
    the lowest pressure which allows injection to prevent exceeding the 
    fuel cladding temperature limit. The new allowable values were 
    selected to lie within the upper and lower limits to ensure there 
    will be no change in the required logic or functions of the Core 
    Spray and LPCI systems. These new values do not affect the LOCA or 
    its ``limiting fault'' frequency of occurrence and do not introduce 
    any new accidents or malfunctions of equipment important to safety. 
    Since they do not affect the LOCA, they do not change the 
    probability of occurrence of the LOCA. The new allowable values do 
    not change the logic or function of the reactor vessel low pressure 
    permissive. These new values simply provide the basis for which the 
    associated pressure
    
    [[Page 17029]]
    
    instruments are to be set to ensure proper operation of Core Spray 
    and LPCI within the design pressures as described above. Therefore, 
    the change in allowable values does not increase the probability of 
    occurrence or the consequences of an accident or malfunction of 
    equipment important to safety.
        Based upon the analysis presented above, PP&L [PP&L, Inc.] 
    concludes that the proposed action does not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This proposal does not create the probability of a new or 
    different type of accident from any accident previously evaluated. 
    The new allowable values do not change any plant systems, 
    structures, or components, nor do they change any existing or create 
    any new Core Spray and LPCI logic or functions. The new allowable 
    values were selected to ensure the required operation of the Core 
    Spray and LPCI systems within the design pressures described above.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The change does not involve a reduction in the margin of safety. 
    Technical Specification Bases Section B3.3.5.1 9 (ECCS 
    Instrumentation) identifies that the low reactor steam dome pressure 
    signals are used as permissives for operation of the low pressure 
    ECCS subsystems. The new allowable values were selected so to not 
    impact the logic, redundancy, operability or surveillance 
    requirements for these subsystems. The new allowable values maintain 
    the margin requirements that the Core Spray and LPCI system 
    pressures such that they do not exceed their system maximum design 
    pressures and that system pressures are high enough to ensure that 
    the ECCS injection prevents the fuel peak cladding temperature from 
    exceeding the limits of 10CFR50.46.
    
        The margin of safety is unaffected by the proposed changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(C) are 
    satisfied. Therefore, the NRC staff proposed to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Bryan A. Snapp, Esquire, Assoc. General 
    Counsel, PP&L, Inc., 2 North Ninth St., GENTW3, Allentown, PA 18101-
    1179.
        NRC Project Director: Elinor G. Adensam.
    
    PP&L, Inc., Docket No. 50-387, Susquehanna Steam Electric Station, Unit 
    1, Luzerne County, Pennsylvania
    
        Date of amendment request: March 12, 1999.
        Description of amendment request: This proposed amendment would 
    revise the minimum critical power ratio safety limit in Technical 
    Specification (TS) Section 2.1.1.2. Also, the proposed amendment would 
    modify the references in TS Section 5.6.5 in order to include only 
    those references that directly support the generation of the Core 
    Operating Limit and to remove the reference for the Lead Use 
    Assemblies, which will be discharged during the next Unit 1 refueling 
    outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The applicable sections of the FSAR are Chapters 4.4 and 15. 
    FSAR Chapter 4.4 describes the MCPR Safety Limit, and Chapter 15 
    describes the transient and accident analyses. The reference to be 
    added to Section 5.6.5 of the Unit 1 Technical Specifications 
    describes a NRC approved critical power correlation for 
    ATRIUMTM-10 fuel. This correlation is appropriate for use 
    in conservative methodologies for generating MCPR Safety Limits and 
    MCPR Operating Limits to assure safe operation of Unit 1 with 
    ATRIUMTM-10 fuel. A discussion of the impact of the 
    proposed Technical Specification change is provided below.
        The proposed change in critical power correlation does not 
    physically affect the plant or its systems. Thus, it does not 
    increase the probability of an accident previously evaluated.
        A Unit 1 Cycle 12 MCPR Safety Limit analysis was performed for 
    PP&L by SPC. This analysis used NRC approved methods described in 
    ANF-524(P)(A), Revision 2 and Supplement 1 Revision 2. These methods 
    will be used each cycle to calculate the Unit 1 Safety Limits. For 
    Unit 1 Cycle 12, the critical power performance of the 9 x 9-2 and 
    ATRIUMTM-10 fuel was determined using the NRC approved 
    ANFB and ANFB-10 correlations, respectively. The SAFETY LIMIT MCPR 
    calculations statistically combine uncertainties on feedwater flow, 
    feedwater temperature, core flow, core pressure, core power 
    distribution, and uncertainties in the Critical Power Correlation. 
    The SPC analysis used cycle specific power distributions and 
    calculated MCPR values such that at least 99.9% of the fuel rods are 
    expected to avoid boiling transition during normal operation or 
    anticipated operational occurrences. The resulting two-loop and 
    single-loop MCPR Safety Limits are included in the proposed 
    Technical Specification change. Thus, the cladding integrity and its 
    ability to contain fission products are not adversely affected.
        Analyses of the Single Loop Pump Seizure accident with the NRC 
    approved ANFB-10 correlation for ATRIUMTM-10 fuel 
    (Reference 1) will be performed to demonstrate that the NRC 
    acceptance criterion (i.e., small fraction of 10CFR100 dose limits) 
    is met. Analyses will also be performed to validate the conclusion 
    that two-loop transients are more severe than those events analyzed 
    in single-loop operation.
        Changes to Section 2.1.1.2 reflect the change from a flow 
    dependent MCPR Safety Limit to a single value MCPR Safety Limit for 
    two-loop operation and single-loop operation.
        Changes to Reference 5.6.5 delete the methodology used for 
    critical power analyses for ATRIUMTM-10 fuel and add the 
    NRC approved ANFB-10 methodology to the list of approved 
    methodologies. Other changes in Reference 5.6.5 are administrative 
    in nature because they delete references not directly related to the 
    generation of Core Operating Limits. No new analysis approaches are 
    used due to these changes.
        Changes to BASES Sections 2.1.1 and 3.2.2 reflect the inclusion 
    of the ANFB-10 critical power correlation. The range of the 
    applicability of the ANFB-10 is valid for pressures > 571 psia and 
    bundle mass fluxes > 0.115  x  10\6\ lb/hr-ft \2\. These values 
    assure that a valid CPR calculation will result at or above 25% of 
    rated core thermal power, that is, reactor steam dome pressure 
     785 psig and core flow  10 Mlbm/hr.
        Changes to BASES Sections 3.2.1, 3.2.2, 3.2.3, and 3.2.4 reflect 
    the removal of Reference 7 for the ABB LUAs, since the four LUAs 
    will be discharged from Unit 1 during the Unit 1 11th Refueling and 
    Inspection Outage.
        The consequences of transients and accidents will remain within 
    the criteria approved by the NRC. The methodology used to perform 
    the analyses has been previously approved by the NRC. Thus, analysis 
    results using the new methodology will continue to provide assurance 
    that the reactor will perform its design safety function during 
    normal operation and design basis events. Therefore, the proposed 
    action does not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the Unit 1 Technical Specifications 
    (MCPR Safety Limits, removal of methodology references not directly 
    supporting the generation of Core Operating Limits, removal of the 
    two references describing previously approved methodology for 
    applying ANFB to ATRIUMTM-10 fuel, removal of the ABB LUA 
    reference, and inclusion of the ANFB-10 correlation reference) do 
    not require any physical plant modifications, physically affect any 
    plant components, or entail changes in plant operation. Removal of 
    the Unit 1 Cycle 11 footnote allows Unit 1 Cycle 12 and future cycle 
    operation with NRC
    
    [[Page 17030]]
    
    approved methodology. Thus, the proposed change does not create the 
    possibility of a previously unevaluated operator error or a new 
    single failure. The consequences of transients and accidents will 
    remain within the criteria approved by the NRC. Therefore, the 
    proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The applicable Technical Specification Sections include 2.1.1.2 
    and 5.6.5.
        The changes to the Unit 1 Technical Specifications discussed in 
    Item 1 above do not require any physical plant modifications, 
    physically affect any plant components, or entail changes in plant 
    operation. Therefore, the proposed change will not jeopardize or 
    degrade the function or operation of any plant system or component 
    governed by Technical Specifications. The consequences of transients 
    and accidents will remain within the criteria approved by the NRC. 
    The proposed MCPR Safety Limits and use of the ANFB-10 critical 
    power correlation described in the reference added to Section 5.6.5 
    do not involve a significant reduction in the margin of safety as 
    currently defined in the Bases of the applicable Technical 
    Specification sections.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Bryan A. Snapp, Esquire, PP&L, Inc., 2 North 
    Ninth St., Allentown, PA 18101.
        NRC Project Director: Elinor G. Adensam.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: March 2, 1999.
        Description of amendment request: The proposed amendment would 
    clarify the use of a ``check valve with flow through the valve 
    secured'' as a means to isolate an affected containment penetration 
    (i.e., a penetration with an inoperable penetration barrier) in 
    Technical Specification 3.6.3 Action b.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change does not involve an increase in the 
    probability or consequences of an accident previously evaluated. The 
    proposed change does not involve any hardware changes. The proposed 
    change will clarify Technical Specification 3.6.3 Action b to allow 
    the use of a check valve with the flow through the valve secured as 
    a means to isolate an inoperable containment penetration. This 
    change is consistent with the changes identified in NUREG-1431, 
    ``Improved Standard Technical Specifications for Westinghouse 
    Plants'', Specification 3.6.3 (Containment Isolation Valves), which 
    identifies check valves with flow through the valve secured as a 
    type of deactivated automatic valve, and with 10 CFR 50 Appendix A 
    General Design Criteria 55 and 56, which include the use of check 
    valves as ``automatic isolation valves''. The proposed change will 
    not affect the containment isolation valve OPERABILITY requirements 
    or associated isolation time limits established in the 
    Specifications. Therefore the proposed change will not affect any 
    safety margin or safety limit applicable to the facility. Therefore 
    no increase in the probability or consequences of any accident 
    previously evaluated will occur.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change will clarify Technical Specification 3.6.3 
    Action b to allow the use of a check valve with the flow through the 
    valve secured as a means to isolate an inoperable containment 
    penetration. The proposed change will not involve any physical 
    change to plant systems, structures, or components (SSC). This 
    change is consistent with the changes identified in NUREG-1431, 
    ``Improved Standard Technical Specifications for Westinghouse 
    Plants'', Specification 3.6.3 (Containment Isolation Valves), which 
    identifies check valves with flow through the valve secured as a 
    type of deactivated automatic valve, and with 10 CFR 50 Appendix A 
    General Design Criteria 55 and 56, which include the use of check 
    valves as ``automatic isolation valves''. The proposed change only 
    provides clarification to the existing Specification 3.6.3, and will 
    not affect the established containment isolation valve OPERABILITY 
    requirements or associated isolation time limits. Since the proposed 
    change does not impact operation of the facility as presently 
    approved, no possibility exists for a new or different kind of 
    accident from those previously evaluated.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change will clarify Technical Specification 3.6.3 
    Action b to allow the use of a check valve with the flow through the 
    valve secured as a means to isolate an inoperable containment 
    penetration. This change is consistent with the changes identified 
    in NUREG-1431, ``Improved Standard Technical Specifications for 
    Westinghouse Plants'', Specification 3.6.3 (Containment Isolation 
    Valves), which identifies check valves with flow through the valve 
    secured as a type of deactivated automatic valve, and with 10 CFR 50 
    Appendix A General Design Criteria 55 and 56, which include the use 
    of check valves as ``automatic isolation valves''. The proposed 
    change only provides clarification to the existing Specification 
    3.6.3, and will not affect the established containment isolation 
    valve OPERABILITY requirements or associated isolation time limits. 
    The proposed change does not involve a significant reduction in a 
    margin of safety because the ability to isolate containment in the 
    event of a release of radioactive material to the containment 
    atmosphere or pressurization of the containment will be maintained. 
    The margin of safety is defined by the established containment 
    isolation valve OPERABILITY requirements and associated isolation 
    time limits. The proposed change does not alter these operating 
    restrictions and the margin of safety which assures the ability to 
    isolate containment is not affected.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: George Dick, Acting.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: March 9, 1999.
        Description of amendment request: The amendment request proposes 
    that reference to the Independent Safety Engineering Group be removed 
    from Technical Specification requirements, with supporting changes to 
    the Operations Quality Assurance Plan.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed amendment is a programmatic and administrative 
    change that
    
    [[Page 17031]]
    
    does not physically alter safety-related systems, nor does it affect 
    the way in which safety-related systems perform their functions. The 
    functions assigned to the Independent Safety Engineering Group are 
    addressed by other organizations. Because the design of the facility 
    and system operating parameters are not being changed, the proposed 
    amendment does not involve an increase in the probability or 
    consequences of any accident previously evaluated.
        The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment is a programmatic and administrative 
    change that does not physically alter safety-related systems, nor 
    does it affect the way in which safety-related systems perform their 
    functions. The functions assigned to the Independent Safety 
    Engineering Group are addressed by other organizations. Because the 
    design of the facility and system operating parameters are not being 
    changed, the proposed amendment does not create the possibility of a 
    new or different kind of accident previously evaluated.
        The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed amendment is a programmatic and administrative 
    change that provides assurance that plant operations continue to be 
    conducted in a safe manner. The functions assigned to the 
    Independent Safety Engineering Group are addressed by other 
    organizations. As stated above the proposed amendment does not 
    physically alter safety-related systems, nor does it affect the way 
    in which safety-related systems perform their functions. Because the 
    design of the facility and system operating parameters are not being 
    changed, the proposed amendment does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: George F. Dick, Acting.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: March 15, 1999 (Supplement to October 
    29, 1998).
        Description of amendment request: The proposed amendments were 
    submitted by application dated October 29, 1998, to relocate Technical 
    Specification (TS) 3/4.7.9 requirements for snubbers to the Technical 
    Requirements Manual. The Commission issued a Notice of Consideration of 
    Issuance of Amendments regarding its proposed no significant hazards 
    consideration determination that was published in the Federal Register 
    on December 16, 1998 (63 FR 69346).
        Subsequently, by letter dated March 15, 1999, supplemental 
    information was submitted to include TS 6.10.3.l to be relocated to the 
    Technical Requirements Manual. This information is being noticed to 
    provide for public comment on the issue of no significant hazards 
    consideration.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The supplement to the amendment request relocates the record 
    keeping requirements of Technical Specification 6.10.3.l to the 
    Technical Requirements Manual. The change does not involve a 
    physical alteration of the plant (no new or different type of 
    equipment will be installed) or make changes in the methods 
    governing normal plant operation. The change will not impose 
    different requirements, and adequate control of information will be 
    maintained. This change will not alter assumptions made in the 
    safety analysis and licensing basis.
        The Technical Requirements Manual is incorporated in the South 
    Texas Project Updated Final Safety Analysis Report and will be 
    maintained pursuant to 10 CFR 50.59. In addition, snubber 
    operability is addressed in existing surveillance procedures that 
    are also controlled by 10 CFR 50.59 and subject to the change 
    control provisions imposed by plant administrative procedures, which 
    endorse applicable regulations and standards.
        Therefore, the supplement to the proposed change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The supplement to the amendment request relocates the record 
    keeping requirements of Technical Specification 6.10.3.l to the 
    Technical Requirements Manual. The change does not involve a 
    physical alteration of the plant (no new or different type of 
    equipment will be installed) or make changes in the methods 
    governing normal plant operation. The change will not impose 
    different requirements, and adequate control of information will be 
    maintained. This change will not alter assumptions made in the 
    safety analysis and licensing basis.
        The Technical Requirements Manual is incorporated in the South 
    Texas Project Updated Final Safety Analysis Report and will be 
    maintained pursuant to 10 CFR 50.59. In addition, snubber 
    operability is addressed in existing surveillance procedures that 
    are also controlled by 10CFR50.59 and subject to the change control 
    provisions imposed by plant administrative procedures, which endorse 
    applicable regulations and standards.
        Therefore, the change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The supplement to the amendment request relocates the record 
    keeping requirements of Technical Specification 6.10.3.l to the 
    Technical Requirements Manual. The relocated requirements remain the 
    same as the existing Technical Specifications. The change will not 
    reduce a margin of safety because it has no impact on any safety 
    analysis assumptions. Future changes to the relocated requirements 
    will be evaluated per the requirements of 10CFR50.59.
        Therefore, the supplement will not result in a reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: George F. Dick, Acting.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: February 15, 1999.
        Description of amendment request: The proposed amendment would 
    revise requirements of Technical Specifications Section 6, 
    ``Administrative Controls,'' related to (1) plant manager's 
    responsibilities, (2) plant staff titles and organization, (3) offsite 
    and onsite review committee (4) reportable events, and (5) actions 
    required in event of a safety limit violation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards
    
    [[Page 17032]]
    
    consideration, which is presented below:
    
        The proposed amendment will not change the intent of the TS or 
    decrease WPSC's management support or involvement in activities at 
    the Kewaunee Plant. Furthermore, it will not result in a decrease in 
    the engineering or technical support supplied by the plant staff or 
    the corporate support staff. The proposed changes are administrative 
    in nature. They primarily involve the relocation of existing 
    requirements to owner controlled documents; therefore, there are no 
    significant hazards associated with this change. As an 
    administrative change this will not result in a significant increase 
    in the probability of occurrence or consequences of an accident. As 
    an administrative change this will not create the possibility of a 
    new or different kind of accident from any previously analyzed. This 
    administrative change relocates existing requirements, and 
    therefore, will not involve a significant decrease in the margin of 
    safety.
    
        In addition, the staff analyzed the proposed changes in accordance 
    with the provisions of 10 CFR 50.92. The proposed change will not:
        1. Involve a significant increase in the probability or consequence 
    of an accident previously evaluated.
        The analyses for the previously evaluated accidents are presented 
    in Chapter 14 of the Updated Safety Analysis Report. There are 19 
    postulated accidents addressed therein. The proposed amendment would 
    not affect the safety analysis assumptions or analytical models used 
    for any of these analyses. Also, the calculated dose consequences for 
    analyzed accidents would be unaffected. Therefore the proposed changes 
    do not involve a significant increase in the probability or consequence 
    of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed accident does not involve any physical change to the 
    design of the physicality, or operation of the facility outside the 
    bounds of the existing analyses. Thus, there is no possibility of 
    creating a new or different kind of accident.
        3. Involve a significant reduction in the margin of safety.
        The proposed changes do not involve any physical changes to any of 
    the fission product barriers or to the design or operation of any 
    safety systems. Also, no safety limits, limiting safety systems 
    settings, limiting conditions for operation or testing requirements 
    would be affected. Therefore, the proposed changes do not involve a 
    significant reduction in the margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, WI 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P.O. Box 1497, Madison, WI 53701-1497.
        NRC Project Director: Cynthia A. Carpenter.
    
    Yankee Atomic Electric Company, Docket No. 50-29, Yankee Nuclear Power 
    Station, Franklin County, Massachusetts
    
        Date of amendment request: March 17, 1999.
        Description of amendment request: Licensee submitted a License 
    Amendment request to delete administrative Technical Specification (TS) 
    requirements related to overtime restrictions. The licensee stated it 
    will provide appropriate constraints on excessive overtime in its 
    Administrative Procedures.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed changes are administrative in nature and simply 
    eliminate outdated requirements from the YNPS Technical 
    Specifications. As such the changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The administrative 
    nature of the changes will not affect safety-related systems or 
    components or their mode of operation and therefore, will not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Create the possibility of a new or different accident from 
    any previously evaluated. The proposed changes do not modify any 
    plant systems or components and, therefore, do not create the 
    possibility of a new or different accident from any previously 
    evaluated.
        3. Involve a significant reduction in the margin of safety. The 
    changes are administrative in nature involving the deletion of 
    outdated requirements in the technical specifications; therefore, 
    there will be no reduction in the margin of safety.
    
    Based on the considerations noted above, it is concluded that the 
    proposed changes will not endanger the public health and safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Greenfield Community College, 
    1 College Drive, Greenfield, Massachusetts 01301.
        Attorney for licensee: Thomas Dignan, Esquire, Ropes and Gray, One 
    International Place, Boston, Massachusetts 02110-2624.
        NRC Project Director: Seymour H. Weiss.
    
    Yankee Atomic Electric Company, Docket No. 50-29, Yankee Nuclear Power 
    Station, Franklin County, Massachusetts
    
        Date of amendment request: March 17, 1999.
        Description of amendment request: Licensee submitted a License 
    Amendment request to transfer Technical Specification Sections 6.7--
    Procedures and Programs and 6.9--Record Retention to the Yankee 
    Decommissioning Quality Assurance Program (YDQAP).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed changes are administrative in nature. 
    Administrative requirements in Sections 6.7 and 6.9 of the YNPS 
    Technical Specifications are to be transferred to the YDQAP which is 
    the current location of related administrative requirements. As such 
    the changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The administrative 
    nature of the changes will not affect safety-related systems or 
    components or their mode of operation and therefore, will not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Create the possibility of a new or different accident from 
    any previously evaluated. The proposed changes do not modify any 
    plant systems or components and, therefore, will not create the 
    possibility of a new or different accident from any previously 
    evaluated.
        3. Involve a significant reduction in the margin of safety. The 
    changes are administrative in nature involving the relocation of 
    administrative requirements from one licensing document to another 
    licensing document currently containing related requirements; 
    therefore, there will be no significant reduction in the margin of 
    safety.
    
    Based on the considerations noted above, it is concluded that the 
    proposed changes will not endanger the public health and safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this
    
    [[Page 17033]]
    
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Greenfield Community College, 
    1 College Drive, Greenfield, Massachusetts 01301.
        Attorney for licensee: Thomas Dignan, Esquire, Ropes and Gray, One 
    International Place, Boston, Massachusetts 02110-2624.
        NRC Project Director: Seymour H. Weiss.
    
    Yankee Atomic Electric Company, Docket No. 50-29, Yankee Nuclear Power 
    Station, Franklin County, Massachusetts
    
        Date of amendment request: March 17, 1999.
        Description of amendment request: Licensee submitted a License 
    Amendment request to consolidate management positions and to transfer 
    Technical Specification review and audit functions to the Yankee 
    Decommissioning Quality Assurance Program (YDQAP).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed changes are administrative in nature and reflect a 
    streamlining of the YAEC/YNPS management structure and procedures 
    consistent with the on-going requirement to complete the remaining 
    scope of YNPS decommissioning safely and efficiently. As such the 
    changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The administrative 
    nature of the changes will not affect safety-related systems or 
    components or their mode of operation and therefore, will not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Create the possibility of a new or different accident from 
    any previously evaluated. The proposed changes do not modify any 
    plant systems or components and, therefore, will not create the 
    possibility of a new or different accident from any previously 
    evaluated.
        3. Involve a significant reduction in the margin of safety. 
    Elimination of the Manager of Operations position and the Plant 
    Superintendent position will not eliminate any of the 
    responsibilities or functions currently assigned to these positions. 
    These responsibilities or functions will be reassigned to an 
    appropriately qualified YAEC/YNPS manager, i.e., the Decommissioning 
    Manager. This change and replacement of the PORC and the NSARC 
    review and audit functions with an independent safety review and an 
    IRAC are consistent with the significant reduction in the scope and 
    the complexity of activities at YNPS as the facility moves into the 
    later stages of the decommissioning effort; therefore, there will be 
    no significant reduction in the margin of safety.
    
    Based on the considerations noted above, it is concluded that the 
    proposed changes will not endanger the public health and safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Greenfield Community College, 
    1 College Drive, Greenfield, Massachusetts 01301.
        Attorney for licensee: Thomas Dignan, Esquire, Ropes and Gray, One 
    International Place, Boston, Massachusetts 02110-2624.
        NRC Project Director: Seymour H. Weiss.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of application for amendment: February 24, 1999.
        Brief description of amendment: The amendment would revise 
    Technical Specification Table 3.3-1, ``Reactor Protective 
    Instrumentation,'' Action 2, for Arkansas Nuclear One, Unit No. 2. The 
    proposed change would add a footnote to Action 2 that would allow 
    startup and operation with the functional units associated with the 
    Channel ``D'' ex-core nuclear instrumentation to be maintained in the 
    bypassed or tripped condition following the restart from Refueling 
    Outage 2R13. This footnote is intended to support normal plant 
    operations until such time that the Channel ``D'' ex-core detector 
    assembly can be restored to an operable status.
        Date of publication of individual notice in Federal Register: March 
    8, 1999 (64 FR 11067).
        Expiration date of individual notice: April 7, 1999.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    [[Page 17034]]
    
    CBS Corporation, Docket No. 50-22, Westinghouse Test Reactor, Waltz 
    Mill, Pennsylvania
    
        Date of application for amendment: September 28, 1998 supplemented 
    on November 17, 1998.
        Brief description of amendment: This amendment changes the license 
    to reflect the new legal name of the licensee for the Westinghouse Test 
    Reactor to CBS Corporation.
        Date of issuance: March 25, 1999.
        Effective Date: March 25, 1999.
        Amendment No: 9.
        Facility License No. TR-2: This amendment changes the license.
        Date of initial notice in Federal Register: December 16, 1998, (63 
    FR 69334).
        The Commission has issued a Safety Evaluation for this amendment 
    dated March 25, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document: N/A.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 
    1 and 2, Rock Island County, Illinois
    
    Docket Nos. 50-373 and 50-374, LaSalle County Station, Units 1 and 2, 
    LaSalle County, Illinois
    
        Date of application for amendments: December 17, 1998.
        Brief description of amendments: The amendments revised the 
    respective facility Technical Specifications (TS) by adding a new 
    Limiting Condition for Operations that provided an administrative 
    enhancement by allowing testing required to return equipment to service 
    to be conducted under administrative controls.
        Date of issuance: March 16, 1999.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 172, 167; 184, 181; 132, 117.
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29, DPR-30, 
    NPF-11 and NPF-18.
        The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 27, 1999 (64 FR 
    4153) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 16, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021; for LaSalle, the Jacobs Memorial Library, 815 North 
    Orlando Smith Avenue, Illinois Valley Community College, Oglesby, 
    Illinois 61348-9692.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: August 14, 1998, as 
    supplemented on October 13 and December 23, 1998.
        Brief description of amendments: The amendments revised the 
    Technical Specifications (TSs) to reflect the use of Siemens Power 
    Corporation (SPC) ATRIUM-9B fuel. Specifically, the amendments 
    incorporate the following into the TSs: (1) new methodologies that will 
    enhance operational flexibility and reduce the likelihood of future 
    plant derates; (2) administrative changes that adopt Improved Standard 
    Technical Specification (iSTS) language where appropriate; and (3) 
    changes to the Minimum Critical Power Ratio.
        Date of issuance: March 16, 1999.
        Effective date: Immediately, to be implemented prior to startup of 
    Cycle 9 for Unit 1 and prior to startup of Cycle 8 for Unit 2.
        Amendment Nos.: 131, 116.
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the TSs.
        Date of initial notice in Federal Register: November 4, 1998 (63 FR 
    59588). The December 23, 1998, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    March 16, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Jacobs Memorial Library, 815 
    North Orlando Smith Avenue, Illinois Valley Community College, Oglesby, 
    Illinois 61348-9692.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: August 14, 1998, as 
    supplemented by letters dated October 13, 1998, and December 23, 1998.
        Brief description of amendments: The amendments changed the Quad 
    Cities Technical Specifications (TS) to reflect the use of Siemens 
    Power Corporation (SPC) ATRIUM-9B fuel. Specifically, the amendments 
    incorporate the following into the TS: (a) new methodologies that will 
    enhance operational flexibility and reduce the likelihood of future 
    plant derates; (b) administrative changes that eliminate the cycle-
    specific implementation of ATRIUM-9B fuel and adopt Improved Standard 
    Technical Specification language where appropriate; and (c) changes to 
    the Minimum Critical Power Ratio (MCPR).
        The amendment for Unit 1 also reflects the removal of Unit 1 
    specific pages incorporated into Unit 1 TS by Amendment No. 182 and are 
    no longer applicable. The August 14, 1998, application superseded an 
    August 29, 1997, application in its entirety (63 FR 2274).
        Date of issuance: March 17, 1999.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 185 & 182.
        Facility Operating License Nos. DPR-29, DPR-30: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 9, 1998 (63 
    FR 48258) and November 4, 1998 (63 FR 59588). The October 13, 1998, 
    submittal changed a reference to a recently NRC-approved additive 
    constant uncertainty (ACU) generic methodology for ATRIUM-9B fuel (ANF-
    1125 (P)(A), supplement 1, Appendix E) from Appendix D which provided 
    an interim value for ACU. This change was noticed on November 4, 1998 
    (63 FR 48258). The December 23, 1998, submittal provided additional 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated March 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: November 30, 1998.
        Brief description of amendments: The amendments changed the 
    technical specifications (TSs) by decreasing the Allowed Outage Time 
    (AOT) from 67 days to 14 days for the Safe Shutdown Makeup Pump (SSMP).
        Date of issuance: March 26, 1999.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 186 & 183.
    
    [[Page 17035]]
    
        Facility Operating License Nos. DPR-29 and DPR-30: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 13, 1999 (64 FR 
    2246).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
        Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, 
    Oconee Nuclear Station, Units 1, 2, and 3, Oconee County, South 
    Carolina.
        Date of application of amendments: September 30, 1998.
        Brief description of amendments: The amendments increase the 
    maximum fuel rod internal pressure in the spent fuel pool from 1200 
    pounds per square inch gauge (psig) to 1300 psig by changing the 
    Updated Final Analysis Report (UFSAR) reference to the computer code 
    used to determine the fuel rod internal pressure (TACO3 computer code 
    would be added) in UFSAR Chapter 15. In addition, the amendments 
    justify not increasing the overall effective decontamination factor for 
    iodine as a consequence of a fuel handling accident and change the 
    terminology used in the UFSAR from ``fuel assembly gap gas pressure'' 
    to ``fuel rod internal pressure.''
        Date of Issuance: March 26, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: Unit 1-301; Unit 2-301; Unit 3-301.
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: 
    Amendments authorized change(s) to the FSAR.
        Date of initial notice in Federal Register: November 4, 1998 (63 FR 
    59590).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas.
    
        Date of application for amendment: February 25, 1999.
        Brief description of amendment: This amendment revises Technical 
    Specification (TS) Table 3.3-1, ``Reactor Protective Instrumentation,'' 
    Action 2, for Arkansas Nuclear One, Unit No. 2 (ANO-2). This change 
    adds a footnote to Action 2 that allows startup and operation with the 
    functional units associated with the Channel ``D'' ex-core nuclear 
    instrumentation to be maintained in the bypassed or tripped condition 
    following the restart from Refueling Outage 2R13. This footnote is 
    intended to support normal plant operations until such time that the 
    Channel ``D'' ex-core detector assembly can be restored to an operable 
    status. This footnote will be in effect for a time period not to extend 
    beyond Mid-Cycle Outage 2P99, which is the next planned entry into cold 
    shutdown conditions for ANO-2. A Notice of Enforcement Discretion 
    (NOED) related to TS Table 3.3-1, Action 2, was issued verbally on 
    February 23, 1999. The NOED is documented in a letter dated February 
    25, 1999.
        Date of issuance: March 23, 1999.
        Effective date: As of the date of issuance.
        Amendment No.: 202.
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration (NSHC): Yes (64 FR 11067 dated March 8, 1999). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    NSHC determination. No comments have been received. The notice also 
    provided for an opportunity to request a hearing by April 7, 1999, but 
    indicated that if the Commission makes a final NSHC determination, any 
    such hearing would take place after issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final NSHC determination are contained in a 
    Safety Evaluation dated March 23, 1999.
        Attorney for Licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington DC 20005-3502.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio.
    
        Date of application for amendment: November 2, 1995, and as 
    supplemented by submittal dated January 7, 1999.
        Brief description of amendment: This amendment revises technical 
    specification requirements for handling irradiated fuel in the Primary 
    Containment and the Fuel Handling Building, and selected specifications 
    associated with performing core alterations.
        Date of issuance: March 11, 1999.
        Effective date: March 11, 1999.
        Amendment No.: 102.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62497).
        The supplemental information contained clarifying information and 
    did not change the initial no significant hazards consideration 
    determination and did not change the scope of the original application.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 11, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio.
    
        Date of application for amendment: August 27, 1996, as supplemented 
    by submittals dated April 9, 1997, July 22, 1998, December 3, 1998, and 
    January 18, 1999.
        Brief description of amendment: This amendment revised Technical 
    Specification 3.6.1.3, ``Primary Containment Isolation Valves 
    (PCIVs),'' and 3.6.1.9, ``Main Steam Isolation Valve (MSIV) Leakage 
    Control System (LCS).'' The amendment reflects implementation of the 
    revised accident source term in NUREG-1465, ``Accident Source Terms for 
    Light-Water Nuclear Power Plants'' and permits the licensee to 
    eliminate the MSIV LCS and increase the allowable leak rates of the 
    MSIVs.
        Date of issuance: March 26, 1999:
        Effective date: March 26, 1999.
        Amendment No.: 103.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 7, 1998 (63 FR 
    53958).
        The supplemental information contained clarifying information and 
    did not change the initial no significant hazards consideration 
    determination and did not expand the scope of the original application.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
    
    [[Page 17036]]
    
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio.
    
        Date of application for amendment: October 27, 1998.
        Brief description of amendment: This amendment revised the minimum 
    critical power ratio (MCPR) safety limit contained in TS 2.1.1.2. In 
    addition, the amendment removes a note to TS 2.1.1.2 and a footnote to 
    TS 5.6.5.b that references MCPR safety limit values as cycle specific.
        Date of issuance: March 26, 1999:
        Effective date: March 26, 1999.
        Amendment No.: 104.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 2, 1998 (63 FR 
    66603).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio.
    
        Date of application for amendment: September 9, 1998, as 
    supplemented by submittals dated January 6, March 4, and March 18, 
    1999.
        Brief description of amendment: This amendment revises the design 
    and licensing basis of containment isolation valves in the feedwater 
    system. The amendment revises (1) Surveillance Requirement 3.6.1.3.11 
    of Technical Specification (TS) 3.6.1.3, ``Primary Containment 
    Isolation Valves (PCIVs)'' to exclude the feedwater check valves from 
    the hydrostatic test program, (2) TS 5.5.2, ``Primary Coolant Sources 
    Outside Containment,'' to stipulate that water leakage past the 
    feedwater motor-operated containment isolation valves and the reactor 
    water cleanup system return to feedwater line is added to the program, 
    and (3) TS 5.5.12, ``Primary Containment Leakage Rate Testing 
    Program,'' to state that the feedwater check valves will be tested in 
    accordance with the Inservice Testing Program (TS 5.5.6).
        Date of issuance: March 26, 1999.
        Effective date: March 26, 1999.
        Amendment No.: 105.
        Facility Operating License No. NPF-58: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 21, 1998 (63 FR 
    56262).
        The supplemental information contained clarifying information and 
    did not change the initial no significant hazards consideration 
    determination and did not expand the scope of the original Federal 
    Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida.
    
        Date of application for amendments: August 24, 1998.
        Brief description of amendments: These amendments change the St. 
    Lucie Technical Specifications (TSs) by both removing obsolete license 
    conditions and revising the TSs. The amendments change the TSs to 
    modify the St. Lucie Unit 1 TSs to add components, not previously 
    described in the TSs, to the list of components that comprise an 
    operable control room emergency ventilation system, to modify the Unit 
    1 and Unit 2 TSs surveillance requirements to clarify component 
    operations, not previously described, that must be verified in response 
    to a containment sump recirculation actuation signal, to delete from 
    the facility operating license No. NPF-16 for Unit 2, license condition 
    2.C.19 to reflect the completion of the Unit 1 spent fuel pool re-rack 
    and delete license condition 2.I to reflect the resolution of 
    litigation and to modify license condition 2.B.5 to restore the 
    original syntax of the license condition and license condition 2.F to 
    update the references to current license conditions.
        Date of Issuance: March 17, 1999.
        Effective Date: These amendments shall be implemented within 30 
    days of receipt.
        Amendment Nos.: 160 and 99.
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the TSs.
        Date of initial notice in Federal Register: September 23, 1998 (63 
    FR 50937).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey.
    
        Date of application for amendment: September 3, 1998.
        Brief description of amendment: The amendment revises Technical 
    Specifications 3.4.A.10.e and 3.5.a.2.e to incorporate a Condensate 
    Storage Tank water level of greater than 35 feet.
        Date of Issuance: March 17, 1999.
        Effective date: March 17, 1999, to be implemented within 30 days
        Amendment No.: 204.
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 10, 1999 (64 
    FR 6698).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated March 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Illinois Power Company, Docket No. 50-461, Clinton Power Station, Unit 
    1, DeWitt County, Illinois.
    
        Date of application for amendment: January 20, 1999, as 
    supplemented February 4, 8, and 25, and March 5, 1999.
        Brief description of amendment: The amendment changes the 
    undervoltage relay setpoints.
        Date of issuance: March 26, 1999.
        Effective date: March 26, 1999.
        Amendment No.: 122.
        Facility Operating License No. NPF-62: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1999 (64 FR 
    4474).
        The four supplemental submittals provided additional information 
    and did not change the requested amendment or affect the proposed no 
    significant hazards consideration.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, IL 61727.
    
    [[Page 17037]]
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: April 13, 1998, as supplemented 
    November 5, 1998.
        Brief description of amendment: The proposed amendment would revise 
    the Appendix A Technical Specifications to base the Limiting Condition 
    for Operation for the fuel storage pool water level on a revised 
    analysis of the fuel handling accident and a new analysis for 
    radiological shielding during movement of irradiated fuel.
        Date of issuance: March 16, 1999.
        Effective date: March 16, 1999 (and shall be implemented no later 
    than 30 days).
        Amendment No.: 162.
        Facility Operating License No. DPR-36: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 20, 1998 (63 FR 
    27763). The November 5, 1998, submittal provided additional clarifying 
    information and did not change the initial proposed no significant 
    hazards determination and did not expand the scope of the original 
    application.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 16, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of application for amendment: December 30, 1998.
        Brief description of amendment: The amendment changes Technical 
    Specification (TS) Tables 3.6.14-2 and 4.6.14-2 regarding the noble gas 
    activity monitor channel operability requirement and daily sensor check 
    surveillance requirement to be consistent with the conditions specified 
    in TS 3.1.3.a for operability of the emergency cooling system. Also, 
    this amendment corrects a clerical error in TS 4.6.15.d.
        Date of issuance: March 16, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 165.
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 10, 1999 (64 
    FR 6699).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 16, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: November 19, 1998.
        Brief description of amendment: This amendment changes surveillance 
    frequencies in Technical Specifications 4.8.4.4a and 4.8.4.5a to 
    require testing of the Electrical Protection Assemblies once every 6 
    months with the plant on-line rather than shut down.
        Date of issuance: March 18, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 86.
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: December 30, 1998 (63 
    FR 71970).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 18, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    North Atlantic Energy Service Corporation, et al., Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: May 20, 1998, as supplemented by letter 
    dated January 28, 1999.
        Description of amendment request: Revise Technical Specifications 
    Table 3.3-4 and associated bases to depict a change to the refueling 
    water storage tank low-low level setpoint
        Date of issuance: March 12, 1999.
        Effective date: As of its date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 60.
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications
        Date of initial notice in Federal Register: August 12, 1998 (63 FR 
    43205).
        The supplemental letter provided clarifying information and did not 
    change the staff's proposed no significant hazards determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 12, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: September 9, 1998, as 
    supplemented February 19 and 26, 1999.
        Brief description of amendment: The amendment resolves several 
    previously identified technical specifications (TSs) compliance issues. 
    Specifically, the amendment: (1) changed TS definitions 1.24, ``Core 
    Operating Limits Report,'' 1.27, ``Engineering Safety Feature Response 
    Time,'' and 1.31, ``Radiological Effluent Monitoring and Offsite Dose 
    Calculation Manual (REMODCM)''; (2) changed TS 3.0.2, ``Limiting 
    Condition for Operation,'' by adding a new TS 3.0.6 to the Limiting 
    Condition for Operation TS section; (3) changed TS 4.0.5, 
    ``Surveillance Requirements''; (4) changed the mode applicability of TS 
    3.2.3, ``Total Unrodded Integrated Radial Peaking--FrT''; 
    (5) changed TS 3.3.2.1, ``Engineered Safety Features Actuation System 
    Instrumentation,'' by modifying TS Table 4.3-2 Table Notation (1) which 
    it references; and (6) changed TS 3.4.1.1, ``Reactor Coolant System--
    Reactor Coolant System Vents.'' The associated TS Bases sections were 
    also changed.
        Date of issuance: March 11, 1999.
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment No.: 230.
        Facility Operating License No. DPR-65: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 21, 1998 (63 FR 
    56251).
        The supplemental letters provided clarifying information that did 
    not change the original proposed no significant hazards consideration 
    determination or expand the scope of the original Federal Register 
    notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 11, 1999.
    
    [[Page 17038]]
    
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: July 17, 1998, as supplemented 
    November 10, 1998, and February 11, 1999.
        Brief description of amendment: The amendment revises certain 
    diesel generator (DG) action statements and surveillance requirements 
    to improve overall DG reliability and availability.
        Date of issuance: March 12, 1999.
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance.
        Amendment No.: 231.
        Facility Operating License No. DPR-65: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 12, 1998 (63 FR 
    43207).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 12, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    Northern States Power Company, Docket No. 50-263, Monticello Nuclear 
    Generating Plant, Wright County, Minnesota
    
        Date of application for amendment: November 25, 1997, as 
    supplemented September 25 and November 11, 1998, and January 28, 1999.
        Brief description of amendment: The amendment revises the Technical 
    Specifications for the condensate storage tank (CST) low level suction 
    transfer setpoint for the high pressure coolant injection (HPCI) and 
    reactor core isolation cooling (RCIC) systems to allow removing one CST 
    from service for maintenance.
        Date of issuance: March 19, 1999.
        Effective date: March 19, 1999, with full implementation within 30 
    days.
        Amendment No.: 105.
        Facility Operating License No. DPR-22. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 18, 1998 (63 
    FR 69344) The November 25, 1997, letter and September 25 and November 
    11, 1998, supplements were referenced in the original Federal Register 
    notice. The January 28, 1999, supplement provided an updated Technical 
    Specification page following the incorporation of Amendment 103, issued 
    December 23, 1998. This information was within the scope of the 
    original Federal Register notice and did not change the staff's initial 
    proposed no significant hazards considerations determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 19, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Units 1 and 2, Goodhue County, 
    Minnesota
    
        Date of application for amendments: November 25, 1998.
        Brief description of amendments: The amendments revise Technical 
    Specifications 3.2 and Table 3.5-2B to allow limited inoperability of 
    boric acid storage tank level channels and transfer logic channels to 
    provide for required testing and maintenance of the associated 
    components.
        Date of issuance: March 17, 1999.
        Effective date: March 17, 1999, with full implementation within 30 
    days
        Amendment Nos.: 143 and 134.
        Facility Operating License Nos. DPR-42 and DPR-60. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 16, 1998 (63 
    FR 69345).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 19, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of application for amendments: July 30, 1997, as supplemented 
    by letter dated December 23, 1998.
        Brief description of amendments: The amendments revise the combined 
    Technical Specifications (TS) for the Diablo Canyon Power Plant (DCPP) 
    Unit Nos. 1 and 2 by adding a Limiting Condition for Operation, trip 
    setpoints, and surveillance requirements for a residual heat removal 
    pump trip on refueling water storage tank level-low.
        Date of issuance: March 26, 1999.
        Effective date: March 26, 1999, to be implemented within 30 days 
    from the date of issuance.
        Amendment Nos.: Unit 1--130; Unit 2--128.
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 31, 1997 (62 
    FR 68312).
        The December 31, 1997 supplemental letter provided additional 
    clarifying information, did not expand the scope of the application as 
    originally noted, and did not change the staff's proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of application for amendments: August 26, 1997, as 
    supplemented by letters dated October 14 and November 13, 1997, and 
    January 29, 1998.
        Brief description of amendments: The amendments approve a 
    modification to the Diablo Canyon Power Plant (DCPP), Unit Nos. 1 and 2 
    auxiliary saltwater (ASW) system to bypass approximately 800 feet of 
    Unit 1 and 200 feet of Unit 2 Class 1 ASW pipe, a portion of which is 
    buried below sea level in the tidal zone outside the intake structure.
        Date of issuance: March 26, 1999.
        Effective date: March 26, 1999, and shall be implemented in the 
    next
    
    [[Page 17039]]
    
    periodic update to the FSAR Update in accordance with 10 CFR 50.71(e).
        Amendment Nos.: Unit 1--131; Unit 2--129.
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Final Safety Analysis Report Update.
        Date of initial notice in Federal Register: September 16, 1997 (62 
    FR 48677).
        The October 14 and November 13, 1997, and January 29, 1998, 
    supplemental letters provided additional clarifying information, did 
    not expand the scope of the application as originally noticed, and did 
    not change the staff's original proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: September 25, 1996, as 
    supplemented on October 29, 1997, March 16, 1998, and February 8, 1999.
        Brief description of amendments: The amendments revise the 
    Technical Specifications by revising the voltage and frequency 
    acceptance criteria and the start-timing methodology for the emergency 
    diesel generator surveillance testing.
        Date of issuance: March 23, 1999.
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment Nos: 218 and 200.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    5039).
        The October 29, 1997, March 16, 1998, and February 9, 1999, letters 
    provided clarifying information that did not change the initial 
    proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 23, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments:  September 17, 1998.
        Brief description of amendments: The amendments revise Technical 
    Specification 3/4.8.2, ``Electrical Power Sources--Shutdown,'' for the 
    AC distribution system and the 125-volt and 28-volt DC distribution 
    systems. Specifically, the amendments change the Applicability and 
    Action Statements, if less than the complement of equipment and buses 
    are operable, to eliminate the need to establish containment integrity 
    and to add the action to suspend core alterations, positive reactivity 
    additions, and movement of irradiated fuel assemblies.
        Date of issuance: March 24, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos.: 219 and 201.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 21, 1998 (63 FR 
    56257).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 24, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: April 6, 1995, as supplemented 
    on August 21, 1995. (TS 95-19).
        Brief description of amendments: The amendments change the licenses 
    for Sequoyah Nuclear Plant, Units 1 and 2 by removing the license 
    conditions that reference the post-accident sampling system (PASS). The 
    PASS information has been placed in the Sequoyah Final Safety Analysis 
    Report (FSAR). This Change is consistent with NUREG-1431, ``Standard 
    Technical Specifications--Westinghouse Plants.''
        Date of issuance: March 16, 1999.
        Effective date: March 16, 1999.
        Amendment Nos.: 243 and 233.
        Facility Operating License Nos. DPR-77 and DPR-79: The amendments 
    revise the licenses.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20527). The August 21, 1995, letter provided clarifying information 
    that did not change the original no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 16, 1999.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: April 23, 1998, as supplemented 
    on January 25, 1999.
        Brief description of amendment: The amendment changes the existing 
    requirements for the Residual Heat Removal Service Water (RHRSW), 
    Station Service Water (SSW) and Alternate Cooling Tower Systems (ACS) 
    as identified in Technical Specifications (TSs) 4.5.C and 3/4.5.D.
        Specifically, the changes are as follows:
        (1) Specifications 3.5.D.3 and 4.5.D.3: This requirement is revised 
    to delete the existing allowance for 7 days of operation after both SSW 
    subsystems are made or found to be inoperable.
        (2) Specification 4.5.C.1 and Specification 4.5.D.1: These 
    requirements have been revised to relocate testing information related 
    to pump flow and pressure testing characteristics for the RHRSW and SSW 
    Systems, respectively, to the Technical Requirements Manual.
        (3) Specifications 3.5.D.1, 3.5.D.2, 3.5.D.3, 4.5.D.2, 4.5.D.3, and 
    associated Bases: All references to SSW ``subsystem'' have been 
    replaced by ``essential equipment cooling loop'' to more accurately 
    reflect the Vermont Yankee design and operation. In addition, certain 
    operability clarifications have been made to the Bases relative to 
    affected Specifications.
        (4) Bases for Specification 3.5.D: The Bases have been revised to 
    omit statements that imply that the ACS could provide adequate heat 
    removal following a postulated accident. Other Bases additions have 
    been made that include certain operability clarifications relative to 
    affected Specifications.
        Date of Issuance: March 11, 1999.
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 169.
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
    
    [[Page 17040]]
    
        Date of initial notice in Federal Register: February 10, 1999 (64 
    FR 6713).
        The January 25, 1999, supplement did not affect the original 
    proposed no significant hazards consideration.
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated March 11, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, Vermont 05301.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 20, 1998, as supplemented by 
    letters dated May 28, June 30, August 28, September 4, November 20, and 
    December 8, 1998.
        Brief description of amendment: The amendment revised the technical 
    specifications (TS) to support a modification to the plant to increase 
    the storage capacity of the spent fuel pool and increase the nominal 
    fuel enrichment to 5% weight percent of U-235. The amendment also 
    revised the TS to allow the storage of an additional 279 assemblies in 
    the cask loading pit.
        Date of issuance: March 22, 1999.
        Effective date: March 22, 1999, to be fully implemented no later 
    than December 31, 1999, except that the racks in the cask loading pit 
    may be installed at a future time after the completion of the next 
    refueling outage.
        Amendment No.: 120.
        Facility Operating License No. NPF-42: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 13, 1998 (63 FR 
    37601). The June 30, August 28, September 4, November 20, and December 
    8, 1998, supplemental letters provided additional clarifying 
    information, did not expand the scope of the application as originally 
    noticed, and did not change the staff's proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 22, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: February 4, 1998, as supplemented by 
    letter dated October 20, 1998.
        Brief description of amendment: The amendment revises the 
    requirements in Technical Specification Tables 3.3-3, 3.3-4 and 4.3-2 
    regarding the engineered safety features actuation system (ESFAS) 
    Functional Unit 6.f, and adds a note to Table 4.3-2 to clarify the 
    verification of time delays associated with ESFAS Functional Units 8.a 
    and 8.b.
        Date of issuance: March 23, 1999.
        Effective date: March 23, 1999, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 121.
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 25, 1998 (63 FR 
    14491). The October 20, 1998, supplemental letter provided additional 
    clarifying information, did not expand the scope of the application as 
    originally noticed and did not change the staff's original proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated March 23, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
        Dated at Rockville, Maryland, this 31st day of March 1999.
    
        For the Nuclear Regulatory Commission.
    Suzanne C. Black,
    Acting Director, Division of Licensing Project Management, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 99-8503 Filed 4-6-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
3/25/1999
Published:
04/07/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-8503
Dates:
March 25, 1999.
Pages:
17021-17040 (20 pages)
PDF File:
99-8503.pdf