98-9040. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 63, Number 67 (Wednesday, April 8, 1998)]
    [Notices]
    [Pages 17219-17242]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-9040]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 16, 1998, through March 27, 1998. The 
    last biweekly notice was published on March 25, 1998.
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By May 8, 1998, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the
    
    [[Page 17220]]
    
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: February 11, 1998.
        Description of amendment request: The proposed amendment would 
    modify the Pilgrim Nuclear Power Station (PNPS) Updated Final Safety 
    Analysis Report (UFSAR) Section 10.7, Salt Service Water System, by 
    identifying that certain single active failures do exist that could 
    leave the Salt Service Water (SSW) system in a configuration with one 
    SSW pump serving both SSW trains through open crossover (division) 
    valves for the first 10 minutes of an accident.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        Operation with one (1) SSW pump supplying two (2) SSW trains is not 
    an accident or transient precursor and does not prevent the [Reactor 
    Building Closed Cooling Water] RBCCW system from providing adequate 
    cooling during an accident. Core cooling requires no SSW for the first 
    ten minutes, and no containment cooling is assumed for the first ten 
    minutes. Pump testing has proved no SSW pump damage will result from 
    this configuration so there will be no effect on the containment 
    cooling function. The current licensing basis includes operator action 
    after ten minutes to align the SSW system to achieve containment 
    cooling. This amendment does not affect operator action after ten 
    minutes since pump and valve manipulations are already required to 
    align containment cooling. Therefore, the changes do not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The SSW system operating modes are not accident precursors. They 
    cannot influence the types of accidents that can occur. The SSW pumps 
    can withstand operation under the full range of conditions and for the 
    time periods considered under a one pump, two train system 
    configuration with no adverse effects. The SSW system is properly 
    designed as a common header arrangement with five (5) pumps in which 
    any combination of one to five pumps may operate without damaging 
    effects.
        3. The proposed amendment does not involve a significant reduction 
    in the margin of safety.
        Operation with one (1) SSW pump supplying two (2) SSW trains does 
    not impact the ability to provide adequate core or containment cooling 
    during an accident. Although SSW system flow will be diminished during 
    the first ten minutes of the accident, no system flow at all is needed 
    at that time. The current licensing basis credits operator action after 
    ten minutes to align the [Residual Heat Removal] RHR, RBCCW, and SSW 
    systems for containment cooling.
    
    [[Page 17221]]
    
    Operators are expected to isolate the SSW loops or start additional SSW 
    pumps as necessary given the existing specific conditions.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Cecil O. Thomas.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: February 20, 1998.
        Description of amendment request: The proposed amendment would 
    change the Pilgrim Nuclear Power Station Technical Specification (TS) 
    3/4.5.B and its Bases to incorporate the ultimate heat sink (UHS) 
    temperature of 75 deg.F, as required by Amendment No. 173. The 
    introduction of a UHS temperature restriction requires new 
    specifications, actions, and surveillances for the salt service water 
    system.
        The amendment would also replace existing Specification 3.5.B 
    ``Containment Cooling System'' with new Specification 3/4.5.B.1 
    ``Residual Heat Removal (RHR) Suppression Pool Cooling,'' 3/4.5.B.2 
    ``Residual Heat Removal (RHR) Containment Spray,'' 3/4.5.B.3 ``Reactor 
    Building Closed Cooling Water (RBCCW) System,'' and 3/4.5.B.4 ``Salt 
    Service Water (SSW) System and Ultimate Heat Sink (UHS).'' The proposed 
    new subsections will more clearly define the various subsystems that 
    comprise the containment cooling system and the operating states in 
    which they are applicable. The proposed changes also provide clarity 
    with respect to the application of limiting conditions of operation 
    (LCOs), actions, completion times, and surveillances for the 
    containment cooling subsystems.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Operation of PNPS in accordance with the proposed change will not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated because of the following:
    Administrative Changes
        These proposed changes (editorial rewording, reformatting, 
    repagination, and renumbering) are made to restructure the section, 
    accounting for the new specifications replacing Specification 3/4.5.B. 
    These proposed administrative changes do not alter any existing 
    requirements.
    Technical Changes--More Restrictive
        The proposed changes provide more stringent requirements than 
    previously existed in the Technical Specifications. The more stringent 
    requirements provide greater assurance that the affected systems will 
    remain capable of providing the safety functions assumed in design 
    basis accidents and transients. If anything, the new requirements may 
    decrease the probability or consequences of an analyzed event. The 
    change will not alter assumptions relative to mitigation of an accident 
    or transient event. The more restrictive requirements will not alter 
    the operation of process variables, structures, systems, or components 
    as described in the safety analyses.
    Technical Changes--Relocations
        This proposed change relocates requirements from the Technical 
    Specifications to the Inservice Testing (IST) Program. The (IST) 
    Program documents containing the relocated requirements must be 
    maintained using the provisions of 10 CFR 50.55a and 10 CFR 50.59. 
    Since any changes to the (IST) Program documents will be evaluated per 
    10 CFR 50.55a and 10 CFR 50.59, no increase in the probability or 
    consequences of an accident previously evaluated will be allowed 
    without NRC review.
    Technical Changes--Less Restrictive
        This change relaxes the current requirements to declare the 
    affected RBCCW subsystem inoperable when one of the required RBCCW 
    pumps is inoperable. Since the RBCCW system is not assumed as an 
    initiator of any analyzed event, the proposed change will not affect 
    the probability of an accident occurring. The safety function of the 
    RBCCW system is to support the operability of the RHR suppression pool 
    cooling and spray functions, and component cooling for the RHR and core 
    spray pumps, and area coolers. With one required RBCCW pump inoperable, 
    the remaining pump in the affected subsystem is capable of supporting 
    the component cooling requirements for the RHR and core spray pumps, 
    and area coolers, and the remaining OPERABLE subsystem is capable of 
    supporting the suppression pool cooling and spray functions.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Operation of PNPS in accordance with the proposed change will not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated because of the following:
    Administrative Changes
        The proposed changes do not involve a physical alteration of the 
    plant (no new or different type of equipment will be installed) or 
    changes in methods governing plant operation. The proposed changes will 
    not impose any new or different requirements or eliminate any existing 
    requirements.
    Technical Changes--More Restrictive
        The proposed more restrictive requirements will not alter the plant 
    configuration (no new or different type of equipment will be installed) 
    or change methods governing plant operation. The change does impose 
    different requirements. However, the changes are consistent with 
    assumptions made in the safety analyses.
    Technical Changes--Relocations
        This change relocates requirements to the (IST) Program. This 
    change will not alter the plant configuration (no new or different type 
    of equipment will be installed) or changes in methods governing plant 
    operation. This change will not impose different requirements, and 
    adequate control of information will be maintained. This change will 
    not alter assumptions made in the safety analysis.
    Technical Changes--Less Restrictive
        The proposed change will not involve any physical changes to plant 
    systems, structures, or components (SSC), or the manner in which these 
    systems are operated, maintained, modified, tested, or inspected.
        3. Does this change involve a significant reduction in a margin of 
    safety?
    
    [[Page 17222]]
    
    Administrative Changes
        Operation of PNPS in accordance with the proposed change will not 
    involve a significant reduction in a margin of safety because of the 
    following: safety analysis margin of safety.
        The changes are administrative in nature and do not involve any 
    technical changes. Since no technical changes (either actual or 
    interpretational) were made, there is no impact on any safety analysis 
    margin of safety.
    Technical Changes--More Restrictive
        The proposed more restrictive requirements will not alter 
    assumptions relative to mitigation of an accident or transient event or 
    alter the operation of process variables, structures, systems, or 
    components as described in the safety analyses.
    Technical Changes--Relocations
        This change relocates requirements from the Technical 
    Specifications to the Inservice Testing (IST) Program. The requirements 
    to be transposed to the IST program are the same as the existing 
    Technical Specifications. Since any changes to the (IST) Program 
    documents will be evaluated per 10 CFR 50.55a and 10 CFR 50.59, no 
    reduction in margin of safety previously approved will be allowed 
    without NRC review.
    Technical Changes--Less Restrictive
        The 7 day completion time is consistent with the completion times 
    for one inoperable loop of suppression pool cooling system or 
    containment spray system, and the remaining pump in the affected 
    subsystem is capable of supporting the component cooling requirements 
    for the RHR and core spray pumps, and area coolers.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W.S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, Massachusetts 02199.
        NRC Project Director: Cecil O. Thomas.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: March 12, 1998.
        Description of amendment request: The proposed amendment revises 
    Technical Specification (TS) 3/4.9.12, ``Fuel Handling Building 
    Emergency Exhaust System.'' Specifically, Harris Nuclear Plant (HNP) 
    proposes to delete Surveillance Requirement 4.9.12.d.4, which requires 
    verifying that the filter cooling bypass valve for the Fuel Handling 
    Building Emergency Exhaust System is locked in the balanced position at 
    least once per 18 months.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        Fuel Handling Building Emergency Exhaust System (FHBEES) is not an 
    accident initiating system as described in the Final Safety Analysis 
    Report. The proposed change allows the elimination of the filter 
    cooling bypass flowpath for FHBEES units. Engineering calculations were 
    performed which demonstrate this filter cooling path is not required to 
    mitigate the consequences of a fuel handling accident.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        FHBEES is a ventilation system designed to limit off-site dose 
    releases in the event of a fuel handling accident. FHBEES is not an 
    accident initiating system as described in the Final Safety Analysis 
    Report [FSAR]. The proposed change ensures the seismic and safety 
    classification is maintained while not affecting another Structure, 
    System, or Component.
        Therefore, the proposed change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant reduction 
    in the margin of safety.
        The proposed change to FHBEES does not affect any of the parameters 
    that relate to the margin of safety as described in the Bases of the TS 
    or the FSAR. Accordingly, NRC Acceptance Limits are not affected by 
    this change.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Pao Tsin Kuo, Acting Director.
    
    Consumers Energy Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of amendment request: September 3, 1997, as supplemented March 
    13, 1998.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to delete snubber operability 
    requirements (Change A), action requirements for inoperable snubbers 
    (Change B), and snubber testing requirements (Change E). The snubber 
    testing requirements would be relocated to the Palisades Operating 
    Requirements Manual (ORM). Each proposed change has been classified by 
    the licensee as either Administrative, More Restrictive, or Less 
    Restrictive.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        1. Administrative Change (Change A):
        ``Administrative'' changes make wording changes which clarify 
    existing TS requirements, without affecting their technical content. 
    Since ``Administrative'' changes do not alter the technical content of 
    any requirements, they cannot involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
    
    [[Page 17223]]
    
        2. More Restrictive Change (Change B):
        ``More Restrictive'' changes only add new requirements, or revise 
    existing requirements to result in additional operational restrictions. 
    The TS, with all ``More Restrictive'' changes incorporated, will still 
    contain all of the requirements which existed prior to the changes. 
    Therefore, ``More Restrictive'' changes cannot involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        3. Less Restrictive Change (Change E):
        Change E deletes the TS requirements for snubber testing, but adds 
    identical requirements to a document (the ORM) controlled under 10 CFR 
    50.59.
        10 CFR 50.59 specifically prohibits changes to the facility as 
    described in the safety analysis report, and to procedures described in 
    the safety analysis report (without prior NRC approval) ``if the 
    probability of occurrence or the consequences of an accident or 
    malfunction of equipment important to safety previously evaluated in 
    the safety analysis report may be increased''. Since the conditions 
    which limit changes performed under 50.59 are more restrictive than the 
    conditions which define changes considered to involve a significant 
    hazards consideration, moving of a requirement from the TS to a 
    document which is controlled under 50.59 cannot involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        Do the proposed changes create the possibility of a new or 
    different kind of accident from any previously evaluated?
        1. Administrative Change (Change A):
        ``Administrative'' changes make wording changes which clarify 
    existing TS requirements, without affecting their technical content. 
    Since ``Administrative'' changes do not alter the technical content of 
    any requirements, they cannot create the possibility of a new or 
    different kind of accident from any previously evaluated.
        2. More Restrictive Change (Change B):
        ``More Restrictive'' changes only add new requirements, or revise 
    existing requirements to result in additional operational restrictions. 
    The TS, with all ``More Restrictive'' changes incorporated, will still 
    contain all of the requirements which existed prior to the changes. 
    Therefore, ``More Restrictive'' changes cannot create the possibility 
    of a new or different kind of accident from any previously evaluated.
        3. Less Restrictive Change (Change E):
        Change E deletes the TS requirements for snubber testing, but adds 
    identical requirements to a document (the ORM) controlled under 10 CFR 
    50.59.
        10 CFR 50.59 specifically prohibits changes to the facility as 
    described in the safety analysis report, and to procedures described in 
    the safety analysis report (without prior NRC approval) ``if a 
    possibility for an accident or malfunction of a different type than any 
    evaluated previously in the safety analysis report may be created''. 
    Since the conditions which limit changes performed under 50.59 are more 
    restrictive than the conditions which define changes considered to 
    involve a significant hazards consideration, relocation of a 
    requirement from the TS to a document which is controlled under 50.59 
    cannot create the possibility of a new or different kind of accident 
    from any previously evaluated.
        Do the proposed changes involve a significant reduction in a margin 
    of safety?
        1. Administrative Change (Changes A):
        ``Administrative'' changes make wording changes which clarify 
    existing TS requirements, without affecting their technical content. 
    Since ``Administrative'' changes do not alter the technical content of 
    any requirements, they cannot involve a significant reduction in a 
    margin of safety.
        2. More Restrictive Change (Change B):
        ``More Restrictive'' changes only add new requirements, or revise 
    existing requirements to result in additional operational restrictions. 
    The TS, with all ``More Restrictive'' changes incorporated, will still 
    contain all of the requirements which existed prior to the changes. 
    Therefore, ``More Restrictive'' changes cannot involve a significant 
    reduction in a margin of safety.
        3. Less Restrictive Change (Change E):
        Change E deletes the TS requirements for snubber testing, but adds 
    identical requirements to a document (the ORM) controlled under 10 CFR 
    50.59.
        10 CFR 50.59 specifically prohibits changes to the facility as 
    described in the safety analysis report, and to procedures described in 
    the safety analysis report (without prior NRC approval) ``if the margin 
    of safety as defined in the basis for any technical specification is 
    reduced''. Since the conditions which limit changes performed under 
    50.59 are more restrictive than the conditions which define changes 
    considered to involve a significant hazards consideration, relocation 
    of a requirement from the TS to a document which is controlled under 
    50.59 cannot involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Energy 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: Cynthia A. Carpenter.
    
    Detroit Edison Company, Docket No. 50-16, Enrico Fermi Atomic Power 
    Plant, Unit 1, Monroe County, Michigan
    
        Date of amendment request: December 15, 1997 (Reference NRC-98-
    0023).
        Description of amendment request: The proposed amendment will add a 
    subpart 3 to Part 2.B of the Enrico Fermi Atomic Power Plant, Unit 1 
    (Fermi 1), that would allow the licensee to receive, acquire, possess, 
    use and transfer byproduct material without restriction to chemical or 
    physical form for sample analysis, instrument calibration, or 
    associated with radioactive apparatus, hardware, tools, and equipment, 
    provided the cumulative radioactive material quantity of the byproduct 
    material does not exceed the criteria contained in Section 30.72, 
    Schedule C, ``Quantities of Radioactive Material Requiring 
    Consideration of the Need for an Emergency Plan for Responding to a 
    Release.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration using the standards in 10 CFR 50.92(c). The licensee's 
    analysis is presented below:
        (1) Does the proposed change significantly increase the probability 
    or consequences of an accident previously evaluated?
        The proposed amendment does not involve a significant increase in 
    the probability or consequences of an accident. Using slightly 
    contaminated apparatus or a small non-exempt radioactive source cannot 
    affect the probability of the analyzed sodium or liquid waste 
    accidents. The ability to possess such equipment does not in itself 
    change any methods of handling liquid waste or sodium. Use of
    
    [[Page 17224]]
    
    contaminated equipment could potentially increase the consequences of 
    an accident if it was in use or in the vicinity if an accident occurs. 
    However, the increase in consequences would not be significant due to 
    the limitations on radioactivity content of such equipment. The limit 
    was selected to be that in 10 CFR Part 30.72, Schedule C, as the 
    threshold beyond which offsite emergency plans are required. Since the 
    quantity is below that requiring an offsite emergency plan, even if all 
    the byproduct material allowed to be possessed by the proposed 
    amendment were released during a postulated accident, the consequences 
    would be significantly increased. The quantity contained in any 
    specific piece of contaminated apparatus or a source would be expected 
    to be even less. Therefore, this amendment does not involve a 
    significant increase in the probability or consequences of an accident.
        (2) Will the proposed amendment create the possibility of a new or 
    different kind of accident from any accident previously analyzed?
        The proposed amendment does not create the possibility of a new or 
    different type of accident from any previously evaluated. Allowing 
    possession of contaminated apparatus, tools, or equipment does not 
    change methods of monitoring the facility or operation or surveillance 
    of any system at Fermi 1. While possession of a different source will 
    permit other instruments to be calibrated, source checked, or tested at 
    Fermi 1, testing of instrumentation is routine, ordinary activity. It 
    is not an activity which creates the possibility of a new or different 
    type of accident.
        (3) Will the proposed change significantly reduce the margin of 
    safety at the facility?
        The proposed amendment does not involve a significant reduction in 
    the margin of safety at Fermi 1. No change to any system or the status 
    of any systems or structures, are created by this amendment. Being able 
    to have limited amounts of additional radioactive material at Fermi 1 
    in the form of contaminated apparatus, tools, equipment or hardware or 
    non-exempt radioactive sources will not significantly reduce the margin 
    of safety because a 10 CFR Part 20 program is already in place and the 
    amount of radioactive material is being limited below the amount in 10 
    CFR Part 30.72, Schedule C. For these reasons, this amendment will not 
    significantly reduce the margin of safety at Fermi 1.
        NRC staff has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 50.92(c) are satisfied. 
    Therefore, NRC staff proposes to determine that the amendment request 
    involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
        Attorney for licensee: John Flynn, Esquire, Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Branch Chief: John W. N. Hickey.
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. Lucie 
    Plant, Unit No 2, St. Lucie County, Florida
    
        Date of amendment request: March 3, 1998.
        Description of amendment request: The amendment request proposes to 
    revise the applicability of the St. Lucie Unit 2 technical 
    specifications (TSs) to be consistent with St. Lucie Unit 1 TSs for 
    reactor coolant system (RCS) chemistry. In addition, the amendment 
    request proposes to modify the St. Lucie Unit 2 TSs by making 
    administrative changes to the TS discussion of the criticality design 
    features for fuel storage, and administrative changes to the technical 
    review responsibilities under the cognizance of the Company Nuclear 
    Review Board.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed change to TS 3.4,7 will replace the existing 
    applicability statement of ``At all times'' with ``All MODES.'' This 
    revision will obviate the burden and personnel radiation exposures 
    associated with sampling the RCS for chloride and fluoride 
    concentrations during low temperature, defueled conditions. The 
    existing limits, corrective actions for above limit conditions, and 
    sampling requirements will be applicable for all operational MODES 
    defined in the TS. The proposed applicability will continue to assure 
    consistency with the bases for the RCS chemistry specification, and the 
    potential for occurrence, initial conditions, or consequences of events 
    considered in the safety analyses are not changed. The revisions 
    proposed for TS 5.6.1.a.1 and 6.5.2.9.d are administrative in nature, 
    and assure consistency with the bases for previously approved license 
    amendments. Therefore, operation of the facility in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed amendment will not change the physical plant or the 
    operational MODES defined in the facility license. The changes do not 
    involve the addition of new equipment or the modification of existing 
    equipment, nor do they alter the design of St. Lucie plant systems. 
    Therefore, operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed revision to TS 3.4.7 will not change the existing RCS 
    chemistry requirements that are applicable to the operational MODES 
    defined in the technical specifications. However, the change will allow 
    the chloride and fluoride concentrations to go unmonitored during 
    certain refueling operations when there is no fuel in the reactor 
    vessel. For the limited time intervals associated with this defueled 
    condition, the RCS is depressurized, coolant temperature is near 
    ambient, it is unlikely that the chloride and fluoride concentrations 
    could be significantly increased above the concentrations that existed 
    during MODE 6 prior to the core off-load, and susceptibility to 
    corrosive attack from these halides is, therefore, significantly 
    reduced. The existing bases for the RCS chemistry limiting conditions 
    for operation are not changed, and both the bases and the proposed 
    specification are consistent with the corresponding TS at St. Lucie 
    Unit 1. The proposed revisions to TS 5.6.1.a.1 and TS 6.5.2.9.d are 
    administrative in nature and ensure that descriptions contained therein 
    are consistent with the bases for previously approved license 
    amendments. Therefore, operation of the facility in accordance with the 
    proposed amendment would not involve a significant reduction in a 
    margin of safety.
    
    [[Page 17225]]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Community College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34981-5596.
        Attorney for licensee: M. S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420.
        NRC Project Director: Frederick J. Hebdon.
    
    Florida Power and Light Company, Dockets Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: March 12, 1998
        Description of amendment request: The licensee proposed to amend 
    Turkey Point Unit 3 Facility Operating License DPR-31 to delete license 
    conditions 3.I, ``Steam Generator Repair Program,'' 3.K, ``Integrated 
    Schedule,'' and Section 4 of the Operating License Conditions and 
    renumber Section 5 to Section 4; and to amend Turkey Point Unit 4 
    Facility Operating License DRP-41 to delete license conditions 3.H, 
    ``Steam Generator Repair Program,'' and 3.K, ``Integrated Schedule''. 
    In addition, the proposed amendments would modify Appendix A of 
    Facility Operating Licenses DPR-31 and DPR-41 of the Turkey Point Units 
    3 and 4 Technical Specifications (TS) to delete outdated references 
    from TS Figure 5.1-2, ``Plant Area Map'' and to incorporate a recent 
    organization change in TS 6.5.1.2, and 6.5.3.1.a.
        The proposed changes are administrative in nature because they 
    would remove fulfilled license conditions and outdated TS references, 
    and incorporate an organizational change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed changes are administrative in nature removing 
    fulfilled license conditions, outdated Technical Specification 
    referenced material, and reflecting an organizational change. These 
    amendments will not involve a significant increase in the probability 
    or consequences of an accident previously evaluated because they do not 
    affect assumptions contained in plant safety analyses, the physical 
    design and/or operation of the plant, nor do they affect Technical 
    Specifications that preserve safety analysis assumptions. Therefore, 
    the proposed changes do not affect the probability or consequences of 
    accidents previously analyzed.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The use of the modified specifications cannot create the 
    possibility of a new or different kind of accident from any previously 
    evaluated since the proposed amendments will not change the physical 
    plant or the modes of plant operation defined in the facility operating 
    license. No new failure mode is introduced due to the administrative 
    changes since the proposed changes do not involve the addition or 
    modification of equipment nor do they alter the design or operation of 
    affected plant systems, structures, or components.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The operating limits and functional capabilities of the affected 
    systems, structures, and components are unchanged by the proposed 
    amendments. The organizational change from Services Manager to 
    Protection Services Manager maintained the associated level of 
    management controls and the required qualifications. The proposed 
    changes to the Facility Operating License Conditions and to the 
    Technical Specifications are administrative and do not significantly 
    reduce any of the margins of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Library, Florida International 
    University, University Park Campus, Miami, Florida 33199.
        Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420.
        NRC Project Director: Frederick J. Hebdon.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: March 2, 1998.
        Description of amendment request: The proposed change would revise 
    Technical Specification (TS) 4.5.2.b.1 to delete the requirement to 
    vent the operating chemical volume and control system (CVCS) 
    centrifugal charging pump casing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change does not affect accident initiators or 
    precursors and does not alter the design assumptions affecting the 
    ability of the ECCS [emergency core cooling system] pumps to mitigate 
    the consequences of an accident.
        The proposed change will align the surveillance requirements with 
    the installed system design and normal operating conditions. The intent 
    of the surveillance requirement ensures operability of the CVCS 
    centrifugal charging pumps by verifying that the ECCS pumps and piping 
    is full of water and not subjected to gas binding or hydraulic 
    transients.
        Excluding the venting of the operating CVCS centrifugal charging 
    pump will not effect pump operation nor subject the high head safety 
    injection portion of the ECCS to potential hydraulic transients. 
    Venting the operating pump under a dynamic condition at high system 
    pressure is ineffective.
        The design and installation of the CVCS centrifugal charging pumps 
    is such that significant non-condensable gasses do not collect in the 
    pumps, whether they are running or not. Therefore, it is unnecessary to 
    require periodic pump casing venting to ensure the pumps will remain 
    operable. Venting of the non-operating centrifugal charging pump will 
    continue to be performed, as required by TS 4.5.2b.1.
        Therefore, the proposed change does not involve a significant 
    increase in the
    
    [[Page 17226]]
    
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        The proposed change will not result in new failure modes because no 
    new components or physical changes are involved with this change nor 
    are the components operated in a new or different manner. The proposed 
    change does not alter the ability of the CVCS centrifugal charging 
    pumps to perform their intended function to mitigate the consequences 
    of an initiating event within the acceptance limits assumed in the 
    Updated Final Safety Analysis Report (UFSAR). The proposed change has 
    no impact on component or system interactions, or the plant design 
    basis. Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any previously analyzed.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        There is no impact on equipment design or operation and there are 
    no changes being made to the Technical Specification required safety 
    limits or safety system settings that would adversely affect plant 
    safety. The CVCS centrifugal charging pumps are designed and installed 
    to be self-venting, such that, accumulation, if any, of non-condensable 
    gasses would have no significant impact on pump operation. Since the 
    proposed change will not result in new failure modes, then, the 
    designed margins of safety to minimize/preclude the consequences of a 
    radiological event resulting from a design basis accident remain 
    unchanged. Therefore, the proposed change to eliminate the requirement 
    to vent the operating CVCS centrifugal charging pump casing does not 
    involve a significant reduction in any margin of safety.
        The NRC staff has reviewed the licensee's analysis, and based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Cecil O. Thomas.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: January 30, 1998.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) by relocating pressure-
    temperature (P-T) curves, predicted radiation induced NDTT shift 
    curves, and the low temperature overpressure protection (LTOP) limits 
    and values from the TS to an OPPD controlled document.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes relocate the reactor coolant system (RCS) 
    pressure-temperature (P-T) curves, the predicted radiation induced NDTT 
    shift curve and the low temperature overpressure protection (LTOP) 
    limits to the Fort Calhoun Station Unit No. 1 RCS Pressure-Temperature 
    Limits Report (PTLR).
        Compliance with these curves and limits continues to be required by 
    the Technical Specifications. Changes to the curves and limits will be 
    controlled by TS 5.9.6, and must be in accordance with the NRC and ASME 
    approved methodologies listed there and with 10 CFR 50.59.
        The FCS PTLR in combination with the limitations imposed by the TS, 
    will ensure the integrity of the reactor vessel pressure boundary. 
    Therefore, the proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        There will be no physical alterations to the plant configuration 
    (no new or different equipment is being installed). No changes in 
    operating modes or limits are proposed. The TS retain requirements to 
    maintain the RCS within acceptable operational limits established in 
    accordance with NRC and ASME approved methodologies and assure 
    operability of the LTOP system. As such, the TS will continue to 
    require compliance with the limitations being relocated to the FCS 
    PTLR. Therefore, these proposed changes do not create the possibility 
    of a new or different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        This proposed change to the FCS TS is administrative in nature 
    relocating the P-T curves, NDTT curve, LTOP limits and associated TS 
    requirements to the FCS PTLR in accordance with GL 96-03. Future 
    updates of the FCS PTLR will be conducted under the 10 CFR 50.59 
    process utilizing NRC and ASME approved methodologies (as described in 
    FCS Unit No. 1 PTLR, Rev. 0 and CEOG Task 942, Report CE NPSD-683, Rev. 
    02). Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: January 30, 1998.
        Description of amendment request: The proposed amendment would 
    revise Facility Operating License No. DPR-40 to delete the License Term 
    based on a reevaluation of the end of license fluence.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The previously evaluated accidents affected by this change are 
    limited to the pressurized thermal shock (PTS) events. Vessel 
    embrittlement due to fast neutron associated damage to the limiting 
    beltline region reactor vessel material, which for Fort Calhoun Station 
    is the lower course axial welds, is a
    
    [[Page 17227]]
    
    component in the PTS analysis. The fast neutron, thermal neutron and 
    dpa values of the FCS reactor vessel were recalculated using actual 
    power history values for Cycles 1 through 14 rather than conservative 
    estimates, with the revised BUGLE-93 cross sections from the ENDF/B-VI 
    cross section library to appropriately account for the iron atoms in 
    the thermal shield and a methodology that the NRC has previously 
    approved for neutron fluence calculations performed by Westinghouse. 
    The evaluation included data from the three surveillance capsules (W-
    225, W-265, and W-275) previously removed and analyzed. The evaluation 
    results indicate that the FCS reactor vessel is able to reach current 
    licensed life without exceeding the 10 CFR 50.61 screening criteria for 
    RTPTS of 270 deg.F for limiting axial welds.
        In accordance with 10 CFR 50.61, this assessment must be updated 
    whenever there is a significant change in projected values of 
    RTPTS or upon request for a change in the expiration date of 
    the facility. Since these requirements are contained in 10 CFR 50.61, 
    Section 3.E can be deleted from Operating License No. DPR-40 without 
    resulting in a significant increase in the probability or consequences 
    of any accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change does not physically alter the configuration of 
    the plant and no new or different mode of operation is proposed. 
    Increasing the long term load factor from 0.77 to 0.85 more accurately 
    projects RTPTS by accounting for improvement in FCS 
    operating cycle efficiency. Requirements for assessing and reporting 
    RTPTS are contained in 10 CFR 50.61 and therefore, the 
    proposed change does not create the possibility of a new or different 
    kind of accident from any previously analyzed.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The margin of safety is defined by the draft regulatory guide DG-
    1053 for neutron fluence calculations which requires the methodology to 
    be capable of providing best estimate fluence evaluations within plus 
    or minus 20 percent (1). The analysis shows that the 
    applicable regulatory criteria are met and therefore, the proposed 
    change does not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: March 18, 1998.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications by changing the title of the Shift 
    Supervisor to Shift Manager.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        OPPD proposes to change the title of the Shift Supervisor to Shift 
    Manager. The qualifications required of these individuals and the 
    duties they perform are unchanged. The title of Shift Manager better 
    conveys the appropriate level of responsibility and authority required 
    of the position. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        There will be no physical alterations to the plant configuration 
    (no new or different equipment is being installed). No changes in 
    operating modes or limits are proposed. The qualifications required of 
    these individuals and the duties they perform are unchanged. Therefore, 
    these proposed changes do not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed change in the title of the Shift Supervisor to Shift 
    Manager is strictly administrative. The qualifications required of 
    these individuals and the duties they perform are unchanged. The title 
    of Shift Manager better conveys the appropriate level of responsibility 
    and authority required of the position. Therefore, this change does not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne Count, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for: (1) the standby liquid control (SLC) 
    system that ensures that there is a functioning flow path from the 
    boron injection tank to the reactor pressure vessel, and (2) the scram 
    discharge volume (SDV) that verifies system performance of the vent and 
    drain valves. Specifically, the interval for SLC testing is being 
    increased from once every 18 months to once every 24 months for a 
    maximum interval of 30 months including the 25 percent grace period; 
    and, from once every 36 months to once every 48 months for those 
    surveillances on a staggered test basis. The frequency for testing the 
    SDV vent and drain valves would be increased from once every 18 months 
    to once every 24 months for a maximum interval of 30 months including 
    the 25 percent grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or
    
    [[Page 17228]]
    
    consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the SAR. Therefore, this change will have no impact on the 
    probability of an accident previously evaluated. By changing the 
    surveillance Frequency from 18 months plus grace to a maximum of 30 
    months, the consequences of an accident previously evaluated in the SAR 
    are not significantly increased. This is based on the fact that the 
    evaluation of the subject changes demonstrated that the overall impact, 
    if any, on the systems availability is minimal. Since the impact on the 
    systems is minimal, it can be concluded that the overall impact on the 
    plant accident analysis is negligible. Furthermore, it is shown that 
    the performance history for the subject systems does not indicate any 
    failures which would invalidate the conclusions reached in this 
    evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for performance of channel calibrations on: 
    (1) the reactor protection system (RPS) instrumentation, (2) the source 
    range monitor (SRM) instrumentation, (3) the feedwater-main turbine 
    high-water-level trip instrumentation, (4) the post accident monitoring 
    (PAM) instrumentation, (5) the remote shutdown system instrumentation, 
    (6) the end-of-cycle recirculation pump trip (EOC-RPT) instrumentation, 
    (7) the anticipated transient without scram recirculation pump trip 
    (ATWS-RPT) instrumentation, (8) the emergency core cooling system 
    (ECCS) instrumentation, (9) the rector core isolation cooling (RCIC) 
    system instrumentation, (10) the primary containment isolation 
    instrumentation, (11) secondary containment isolation instrumentation, 
    (12) the control room emergency outside air supply (CREOAS) system 
    instrumentation, (13) the loss of power (LOP) instrumentation, and (14) 
    the RPS electric power monitoring instrumentation. Specifically, the 
    intervals for the associated channel calibration would be increased 
    from either once every 18 months or refueling cycle to once every 24 
    months for a maximum interval of 30 months including the 25 percent 
    grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the SAR. Furthermore, the instrument drift has been 
    evaluated and found to be acceptable for the extended operating 
    cycle[.] Therefore, this change will have no impact on the probability 
    of an accident previously evaluated. By changing the Surveillance 
    Frequency from 18 months plus grace to a maximum of 30 months, the 
    consequences of an accident previously evaluated in the SAR are not 
    significantly increased. This is based on the fact that the evaluation 
    of the subject changes demonstrated that the overall impact, if any, on 
    the systems availability is minimal and instrument drift over the 
    extended operating cycle has been evaluated and found to be acceptable. 
    Since the impact on the systems and from instrument drift is minimal, 
    it can be concluded that the overall impact on the plant accident 
    analysis is negligible. Furthermore, it is shown that the performance 
    history for the subject systems does not indicate any failures which 
    would invalidate the conclusions reached in this evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library,
    
    [[Page 17229]]
    
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for: (1) the integrated leak test of each 
    system listed as a primary coolant source outside containment, and (2) 
    the engineered safety feature filter ventilation systems in the 
    ventillation filter testing program. Specifically, the interval for 
    these tests would be increased from once every 18 months to once every 
    24 months for a maximum interval of 30 months including the 25 percent 
    grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the SAR [safety analysis report]. Therefore, this change 
    will have no impact on the probability of an accident previously 
    evaluated. By changing the Surveillance Frequency from 18 months plus 
    grace to a maximum of 30 months, the consequences of an accident 
    previously evaluated in the SAR are not significantly increased. This 
    is based on the fact that the evaluation of the subject changes 
    demonstrated that the overall impact, if any, on the systems 
    availability is minimal. Because the impact on the systems is minimal, 
    it can be concluded that the overall impact on the plant accident 
    analysis is negligible. Furthermore, it is shown that the performance 
    history for the subject systems does not indicate any failures which 
    would invalidate the conclusions reached in this evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for the AC and DC electrical power system 
    sources. Specifically, the intervals for various functional tests would 
    be increased from once every 18 months to once every 24 months for a 
    maximum interval of 30 months including the 25 percent grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the [safety analysis report] SAR. Therefore, this change 
    will have no impact on the probability of an accident previously 
    evaluated. By changing the Surveillance Frequency from 18 months plus 
    grace to a maximum of 30 months, the consequences of an accident 
    previously evaluated in the SAR are not significantly increased. This 
    is based on the fact that the evaluation of the subject changes 
    demonstrated that the overall impact, if any, on the systems 
    availability is minimal. Because the impact on the systems is minimal, 
    it can be concluded that the overall impact on the plant accident 
    analysis is negligible. Furthermore, it is shown that the performance 
    history for the subject systems does not indicate any failures which 
    would invalidate the conclusions reached in this evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three
    
    [[Page 17230]]
    
    standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would lower the 
    minimum allowable low power setpoint for the control rod block 
    instrumentation rod worth minimzer (RWM) from less than or equal to 20 
    percent rated thermal power (RTP) to less than or equal to 10 percent 
    RTP.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        This change establishes the minimum allowable low power setpoint of 
    the RWM as less than or equal to 10% RTP. This change will not result 
    in a significant increase in the probability of an accident previously 
    evaluated because the Operability of the RWM not considered an 
    initiator for any accidents previously analyzed. This change will not 
    result in a significant increase in the consequences of an accident 
    previously evaluated because, as documented in Amendment 17 to NEDE-
    24011-P-A (GESTAR-II) and the associated NRC SER [safety evaluation 
    report], if core power level exceeds 10% RTP, no control rod pattern 
    can generate rod worths such that the fuel enthalpy would exceed the 
    280 cal/gm fuel enthalpy limit during the worst RDA [rod drop 
    accident].
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SSC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The proposed change does not involve a significant reduction in a 
    margin of safety because, as documented in Amendment 17 to NEDE-24011-
    P-A (GESTAR-II) and the associated NRC SER, if core power level exceeds 
    10% RTP, no control rod pattern can generate rod worths such that the 
    fuel enthalpy would exceed the 280 cal/gm fuel enthalpy limit during 
    the worst RDA.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for the: (1) drywell-to-suppression chamber 
    vacuum breaker leakage test, (2) the primary containment isolation 
    valves functional tests, (3) each reactor instrumentation line excess 
    flow check valve (EFCV) functional tests, (4) the suppression chamber-
    to-drywell vacuum breaker opening setpoint test, (5) the system 
    functional test, visual examination, and heater phase resistance to 
    ground tests for the drywell and suppression chamber hydrogen 
    recombiners, (6) the secondary containment vacuum tests of the standby 
    gas treatment (SGT) subsystem, (7) the seconday containment isolation 
    valves (SCIVs) functional tests, and (8) the SGT subsytem functional 
    tests. Specifically, the intervals for these tests would be increased 
    from once every 18 months to once every 24 months for a maximum 
    interval of 30 months including the 25 percent grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the [Safety Analysis Report] SAR. Therefore, this change 
    will have no impact on the probability of an accident previously 
    evaluated. By changing the Surveillance Frequency from 18 months plus 
    grace to a maximum of 30 months, the consequences of an accident 
    previously evaluated in the SAR are not significantly increased. This 
    is based on the fact that the evaluation of the subject changes 
    demonstrated that the overall impact, if any, on the systems 
    availability is minimal. Since the impact on the systems is minimal, it 
    can be concluded that the overall impact on the plant accident analysis 
    is negligible. Furthermore, it is shown that the performance history 
    for the subject systems does not indicate any failures which would 
    invalidate the conclusions reached in this evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the
    
    [[Page 17231]]
    
    subject systems, it can be concluded that the assumptions in the 
    licensing basis are not impacted by the changes in the subject 
    requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for: (1) the system functional test of the 
    core spray and low pressure coolant injection system, and (2) the high 
    pressure coolant injection (HPCI) and the low pressure HPCI flow test. 
    Specifically, the intervals for system functional tests and response 
    time tests would be increased from once every 18 months to once every 
    24 months for a maximum interval of 30 months including the 25 percent 
    grace period. Additionally, the surveillance test intervals for: (1) 
    the system functional test of the automatic depressurization system 
    (ADS), and (2) the system functional test and low pressure flow test of 
    the reactor core isolation cooling (RCIC) system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the SAR. Therefore, this change will have no impact on the 
    probability of an accident previously evaluated. By changing the 
    Surveillance Frequency from 18 months plus grace to a maximum of 30 
    months, the consequences of an accident previously evaluated in the SAR 
    are not significantly increased. This is based on the fact that the 
    evaluation of the subject changes demonstrated that the overall impact, 
    if any, on the systems availability is minimal. Since the impact on the 
    systems is minimal, it can be concluded that the overall impact on the 
    plant accident analysis is negligible. Furthermore, it is shown that 
    the performance history for the subject systems does not indicate any 
    failures which would invalidate the conclusions reached in this 
    evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test interval for the channel calibration of the reactor 
    coolant system leakage detection instrumentation. The surveillance test 
    interval would be increased from once every 18 months to once every 24 
    months for a maximum interval of 30 months including the 25 percent 
    grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the [S]urveillance 
    Frequency from 18 months to 24 months. The change in [S]urveillance 
    Frequency is not assumed to be an accident initiator for any accidents 
    previously evaluated in the SAR [safety analysis report]. Furthermore, 
    the instrument drift has been evaluated and found to be acceptable for 
    the extended operating cycle. Therefore, this change will have no 
    impact on the probability of an accident previously evaluated. By 
    changing the Surveillance Frequency from18 months plus grace to a 
    maximum of 30 months, the consequences of an accident previously 
    evaluated in the SAR are not significantly increased. This is based on 
    the fact that the evaluation of the subject changes demonstrated that 
    the overall impact, if any, on the systems availability is minimal and 
    instrument drift over the extended operating cycle has been evaluated 
    and found to be acceptable. Since the impact on the systems and from 
    instrument drift is minimal, it can be concluded that the overall 
    impact on the plant accident analysis is negligible. Furthermore, it is 
    shown that the performance history for the subject systems does not 
    indicate any failures which would invalidate the conclusions reached in 
    this evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant
    
    [[Page 17232]]
    
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would remove the 
    operability requirement for the 480 volt engineered safeguards systems 
    bus 0565 undervoltage relay (degraded voltage 65 percent and 92 
    percent) in the loss of power instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes remove from the SSES CTS [Susquehanna Steam 
    Electric Station current technical specifications] items that are 
    informational or implementing details that are adequately and more 
    appropriately controlled by the licensee. Additionally, the proposed 
    changes remove from the SSES CTS items that are contained in the Code 
    of Federal Regulations or other regulatory documents and, therefore, do 
    not need to be repeated in the SSES ITS [improved technical 
    specifications]. These requirements being moved to another controlled 
    document or removed from Technical Specifications are not deleted or 
    changed. Therefore, these changes will not result in any changes to the 
    requirements specified in the SSES CTS, but will reduce the level of 
    regulatory control on the identified requirements. The level of 
    regulatory control has no impact on the probability or the consequences 
    of an accident previously evaluated, therefore, these changes have no 
    impact on the probability or consequences of an accident previously 
    evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes will not involve any physical changes to plant 
    systems, structures, or components (SSC), or the manner in which these 
    SSC are operated, maintained, modified, tested, or inspected. The 
    proposed changes will not impose or eliminate any requirements. 
    Therefore, these changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety as defined in the bases of any Technical 
    Specification is not reduced. The requirements being moved to another 
    controlled document or removed from Technical Specifications remain the 
    same as stated in the SSES CTS. Therefore, no reduction in a margin of 
    safety will be permitted.
        Removal of these items from SSES CTS eliminates the requirement for 
    NRC review and approval of revisions in accordance with 10 CFR 50.92. 
    Elimination of this administrative process does not have a margin of 
    safety that can be evaluated. However, the proposed changes are 
    consistent with the BWR [Boiling-Water Reactor] Standard Technical 
    Specification, NUREG-1433, Rev. 1, which was approved by the NRC. 
    Revising the Technical Specifications to reflect the approved level of 
    detail ensures no significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996.
        Description of amendment request: The change would increase the 
    surveillance test intervals for: (1) the reactor protection system 
    (RPS) instrumentation, (2) the feedwater-main turbine high-water-level 
    trip instrumentation, (3) the end of cycle recirculation pump trip 
    (EOC-RPT) instrumentation, (4) the anticipated transient without scram 
    recirculation pump trip (ATWS-RPT) instrumentation, (5) the emergency 
    core cooling system (ECCS) instrumentation, (6) the reactor core 
    isolation cooling (RCIC) system instrumentation, (7) RPS electric power 
    monitoring system instrumentation, (8) primary containment isolation 
    instrumentation, (9) secondary containment isolation instrumentation, 
    (10) the control room emergency outside air supply (CREOAS) system 
    instrumentation, and (11) the loss of power (LOP) instrumentation. 
    Specifically, the intervals for various logic system functional tests 
    and response time tests would be increased from once every 18 months to 
    once every 24 months for a maximum interval of 30 months including the 
    25 percent grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
    
    [[Page 17233]]
    
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the SAR. Therefore, this change will have no impact on the 
    probability of an accident previously evaluated. By changing the 
    Surveillance Frequency from 18 months plus grace to a maximum of 30 
    months, the consequences of an accident previously evaluated in the SAR 
    are not significantly increased. This is based on the fact that the 
    evaluation of the subject changes demonstrated that the overall impact, 
    if any, on the systems availability is minimal. Since the impact on the 
    systems is minimal, it can be concluded that the overall impact on the 
    plant accident analysis is negligible. Furthermore, it is shown that 
    the performance history for the subject systems does not indicate any 
    failures which would invalidate the conclusions reached in this 
    evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996, and March 2, 1998.
        Description of amendment request: The change would increase the 
    surveillance test interval for the: (1) emergency service water (ESW) 
    system functional test, (2) the control room emergency outside air 
    supply (CREOAS) system functional test and control room pressurization 
    test, and (3) the main turbine bypass system functional and response 
    time tests. Specifically, the interval for these tests would be 
    increased from once every 18 months to once every 24 months for a 
    maximum interval of 30 months including the 25 percent grace period.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes involve a change in the surveillance Frequency 
    from 18 months to 24 months. The change in surveillance Frequency is 
    not assumed to be an accident initiator for any accidents previously 
    evaluated in the [safety analysis report] SAR. Therefore, this change 
    will have no impact on the probability of an accident previously 
    evaluated. By changing the Surveillance Frequency from 18 months plus 
    grace to a maximum of 30 months, the consequences of an accident 
    previously evaluated in the SAR are not significantly increased. This 
    is based on the fact that the evaluation of the subject changes 
    demonstrated that the overall impact, if any, on the systems 
    availability is minimal. Since the impact on the systems is minimal, it 
    can be concluded that the overall impact on the plant accident analysis 
    is negligible. Furthermore, it is shown that the performance history 
    for the subject systems does not indicate any failures which would 
    invalidate the conclusions reached in this evaluation.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        This proposed change will not involve any physical changes to plant 
    systems, structures, or components (SCC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, this change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The margin of safety has not been significantly reduced. Although, 
    there will be an increase in the interval between the subject 
    surveillance tests, the evaluation of the changes demonstrates that 
    there is no evidence of any failures which would impact the subject 
    systems availability. Based on the fact that the increased testing 
    interval has a minimal impact on the subject systems, it can be 
    concluded that the assumptions in the licensing basis are not impacted 
    by the changes in the subject requirements and commitments.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996, and March 2, 1998.
        Description of amendment request: The change would add a 
    surveillance requirement and acceptance criteria to verify the source 
    range monitor (SRM) count rate versus the signal to noise ratio of the 
    SRMs. This change also incorporates a new SRM count rate to signal to 
    noise ratio curve which is based on General Electric Service 
    Information Letter (SIL) 478.
        Basis for proposed no significant hazards consideration 
    determination:
    
    [[Page 17234]]
    
    As required by 10 CFR 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration, which is 
    presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes provide requirements determined to be more 
    conservative than the existing requirements for operation of the 
    facility.
        Therefore, these changes establish or maintain adequate assurance 
    that components are operable when necessary for the prevention or 
    mitigation of accidents or transients and that plant variables are 
    maintained within limits necessary to satisfy the assumptions for 
    initial conditions in the safety analysis. Therefore, these changes do 
    not involve any increase in the probability or consequences of an 
    accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes will not involve any physical changes to plant 
    systems, structures, or components (SSC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, these changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The imposition of more restrictive requirements either has no 
    impact on or increases the margin of plant safety. As provided in the 
    discussion of each of the changes, each change in this category 
    provides additional requirements designed to enhance plant safety. Each 
    of the changes maintains requirements within the safety analyses and 
    licensing basis. Therefore, these changes do not involve a reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388, 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 1, 1996, as supplemented March 2, 
    1998.
        Description of amendment request: The change would reduce the 
    allowable values for the reactor protection system instrumentation 
    scram discharge volume water level--high scram setpoints: (1) for the 
    level transmitter from less than or equal to 88 gallons to less than or 
    equal to 66 gallons, and (2) for the float switch from less than or 
    equal to 88 gallons to less than or equal to 62 gallons in order to be 
    consistent with the design setpoint calculations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes provide requirements determined to be more 
    conservative than the existing requirements for operation of the 
    facility. Therefore, these changes establish or maintain adequate 
    assurance that components are operable when necessary for the 
    prevention or mitigation of accidents or transients and that plant 
    variables are maintained within limits necessary to satisfy the 
    assumptions for initial conditions in the safety analysis. Therefore, 
    these changes do not involve any increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes will not involve any physical changes to plant 
    systems, structures, or components (SSC). The changes in normal plant 
    operation are consistent with the current safety analysis assumptions. 
    Therefore, these changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The imposition of more restrictive requirements either has no 
    impact on or increases the margin of plant safety. As provided in the 
    discussion of each of the changes, each change in this category 
    provides additional requirements designed to enhance plant safety. Each 
    of the changes maintains requirements within the safety analyses and 
    licensing basis. Therefore, these changes do not involve a reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Southern Nuclear Operating Company, Inc, Docket Nos. 50-348 and 50-364, 
    Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, Alabama
    
        Date of amendments request: December 30, 1997.
        Description of amendments request: The proposed amendments would 
    revise the Technical Specification surveillance requirements for the 
    Auxiliary Building and Service Water Building batteries to remove the 
    existing 1.75 volt minimum individual cell voltage associated with the 
    ``service test'' acceptance criterion and replace it with a reference 
    to the battery load profile specified in the Final Safety Analysis 
    Report, Section 8.3.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes to remove and replace specific acceptance 
    criterion in the Technical Specifications with a reference to more 
    detailed and bounding criteria in the FSAR [Final Safety Analysis 
    Report] for service tests on the batteries do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated in the Farley FSAR. The AB [Auxiliary Building] and SWB 
    [Service Water Building] batteries do not initiate any accident. 
    Clarification of testing acceptance criteria does not adversely affect 
    the batteries ability to mitigate the consequences of any accident in 
    the
    
    [[Page 17235]]
    
    Farley FSAR. No new accident initiators are identified as a result of 
    this proposed revision. No new performance requirements for any system 
    that is used to mitigate dose consequences have been imposed by this 
    proposed change. No input assumptions to any dose consequence 
    calculations are affected by this proposed change. All previously 
    reported dose consequences remain bounding. Therefore, the radiological 
    consequences resulting from any accident previously evaluated in the 
    FSAR are not increased.
        2. The proposed changes to remove and replace specific acceptance 
    criterion in the Technical Specifications with a reference to more 
    detailed and bounding criteria in the FSAR for service tests on the 
    batteries do not create the possibility of a new or different kind of 
    accident from any previously evaluated in the Farley FSAR. No new 
    accident scenarios, failure mechanisms or limiting single failures are 
    introduced as a result of the clarifications to the battery service 
    test acceptance criteria. No new challenges to the safety-related AB or 
    SWB 125VDC Distribution Systems have been identified. The 125VDC 
    Systems including the batteries have not been modified. Farley will 
    continue to perform service discharge surveillance tests in accordance 
    with the frequency requirements of the Technical Specifications to 
    demonstrate battery operability. Previously identified accident 
    scenarios remain bounding because the performance requirements of the 
    batteries have not been changed. Therefore, the possibility of a new or 
    different kind of accident is not created.
        3. The proposed changes to remove and replace specific acceptance 
    criterion in the Technical Specifications with a reference to more 
    detailed and bounding criteria in the FSAR for service tests on the 
    batteries do not involve a significant reduction in the margin of 
    safety. All previously established acceptance limits continue to be met 
    for all events since the battery function is to provide power during 
    the time between LOSP [loss of offsite power] & D/G [diesel generator] 
    start and in the event of battery charger failure to mitigate the 
    consequences of any accident scenario. Relocating and clarifying 
    service test acceptance criteria will not invalidate the battery 
    function. There are no physical modifications required to the AB or SWB 
    125VDC Distribution Systems or the batteries. This change will not 
    affect the operation of the batteries or any other safety-related 
    equipment. Applicable values, reflected in the governing electrical 
    design calculations, will be incorporated into the FSAR and will remain 
    or be included in the surveillance test procedures. Since current 
    battery performance acceptance limits will continue to be met, there is 
    no reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama.
        NRC Project Director: Herbert N. Berkow.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: February 13, 1998 (TS 97-04).
        Brief description of amendments: The amendments change the Sequoyah 
    (SQN) Technical Specifications (TS) by relocating the mechanical 
    snubber requirements from Section 3.7.9 of the TS to the SQN Technical 
    Requirements Manual.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority (TVA), the licensee, has provided its analysis of the issue 
    of no significant hazards consideration, which is presented below:
        TVA has concluded that operation of SQN Units 1 and 2, in 
    accordance with the proposed change to the TS, does not involve a 
    significant hazards consideration. TVA's conclusion is based on its 
    evaluation, in accordance with 10 CFR 50.91(a)(1), of the three 
    standards set forth in 10 CFR 50.92(c).
        A. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        The proposed revision to the TS relocates the requirements for SQN 
    snubbers without changing the current requirements and deletes an 
    obsolete License Condition. TVA does not consider the snubbers to be 
    the source of any accident; therefore, this administrative relocation 
    of the requirements and License Condition deletion will not increase 
    the possibility of an accident. The capability of the snubbers will 
    continue to provide the same function in support of accident 
    mitigation. Changes to the relocated requirements will be processed, in 
    accordance with 10 CFR 50.59, to ensure the snubber functions will be 
    properly maintain[ed]. Therefore, the proposed relocation of the 
    snubber requirements and License Condition deletion will not increase 
    the consequences of an accident.
        B. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The SQN safety-related snubbers provide support for mitigation 
    functions associated with previously evaluated accidents and are not 
    the initiator of any accident. The proposed change does not alter the 
    current functions of the snubbers; therefore, it will not create the 
    possibility of a new or different kind of accident.
        C. The proposed amendment does not involve a significant reduction 
    in a margin of safety.
        The requirements for SQN safety-related snubbers are unchanged by 
    the proposed relocation of the requirements to the SQN TRM [Technical 
    Requirements Manual] and the License Condition deletion. The function 
    of the snubbers and surveillances to ensure operability will remain the 
    same as currently required by the TS. Changes to these requirements 
    will be evaluated, in accordance with 10 CFR 50.59, to ensure 
    acceptability and NRC review as required. Therefore, the proposed 
    change will not result in a reduction in a margin of safety.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Project Director: Frederick J. Hebdon.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: February 25, 1998 (TS 97-06).
        Brief description of amendments: The amendments change the Sequoyah
    
    [[Page 17236]]
    
    (SQN) Technical Specifications (TSs) for the emergency diesel 
    generators (D/Gs) by 1) incorporating vendor-recommended changes to the 
    D/G inspection program, 2) revising the D/G surveillance program, and 
    3) changing the allowable D/G steady-state voltage range.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority (TVA), the licensee, has provided its analysis of the issue 
    of no significant hazards consideration, which is presented below:
        TVA has concluded that operation of SQN Units 1 and 2, in 
    accordance with the proposed change to the TSs (or operating 
    license[s]), does not involve a significant hazards consideration. 
    TVA's conclusion is based on its evaluation, in accordance with 10 CFR 
    50.91(a)(1), of the three standards set forth in 10 CFR 50.92(c).
        Part 1--Vendor Recommended Inspections:
        The proposed amendment does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed revision to the TS deletes the requirements for 18-
    month inspections from the TS. TVA does not consider the inspections to 
    be the source of any accident; therefore, this deletion will not 
    increase the possibility of an accident. The D/Gs come within the 
    purview of 10 CFR 50.65, which monitors the effectiveness of 
    maintenance at nuclear power plants. The capability of the D/Gs to 
    provide the required safety function in support of accident mitigation 
    will be unaffected. Therefore, the proposed deletion of the inspection 
    requirements will not increase the consequences of an accident.
        The proposed amendment does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The emergency D/Gs provide support for mitigation functions 
    associated with previously evaluated accidents and are not the 
    initiator of any accident. The proposed change does not alter the 
    current functions of the D/Gs; therefore, it will not create the 
    possibility of a new or different kind of accident.
        The proposed amendment does not involve a significant reduction in 
    a margin of safety.
        The requirements for emergency D/Gs are unchanged by the proposed 
    deletion of the requirements from TSs. The function of the emergency D/
    Gs and surveillances to ensure operability will remain the same as 
    currently required by the TS. NRC will continue to monitor the 
    effectiveness of D/G maintenance as required by 10 CFR 50.65. 
    Therefore, the proposed change will not result in a reduction in a 
    margin of safety.
        Part 2--D/G Online Testing:
        The proposed amendment does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed amendment to allow the load rejection tests and the 
    24-hour D/G endurance run to be conducted during any mode of operation 
    does not significantly increase the probability or consequences of an 
    accident previously evaluated in Chapter 15 of the Final Safety 
    Analysis Report (FSAR) since the capability to safely shutdown the 
    plant following a LOOP [loss of offsite power], LOCA [loss of coolant 
    accident] or LOCA/LOOP coincident with a single failure is maintained 
    throughout the surveillance test. Other aspects of D/G parallel testing 
    (protective devices, risks interactions with offsite power 
    capabilities, and operation) are unaffected by the proposed TS change. 
    Required Class-lE onsite power operability during normal operation, 
    shutdown cooling, LOOP, and accident conditions will be the same.
        Performance of the new SR [Surveillance Requirement] 4.8.1.1.2.g.4 
    requires the D/Gs to be at the same system conditions prior to the test 
    (stabilized operating temperature) as previously required. The LOOP 
    start will continue to be performed as required by SR 4.8.1.1.2.d.4.b.
        In addition, the performance of proposed SRs 4.8.1.1.2.g.1, 
    4.8.1.1.2.g.2, 4.8.1.1.2.g.3, or 4.8.1.1.2.g.4 during Modes 1, 2 or 3 
    will not significantly increase the consequences of perturbations to 
    any of the electrical distribution systems that could result in a 
    challenge to steady state operation or to plant safety systems.
        Performance of proposed SR 4.8.1.1.2.g.1, 4.8.1.1.2.g.2, or 
    4.8.1.1.2.g.3 during Modes 1, 2 or 3 or failure of the surveillance, 
    will not cause, or result in, an anticipated operational occurrence 
    with attendant challenges to plant safety systems that has not been 
    previously analyzed for the existing monthly surveillances.
        Therefore, TVA concludes that the above change does not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The requested changes do not result in a new or different kind of 
    accident from that previously analyzed in SQN's FSAR. The changes 
    propose to eliminate restrictions of the plant operating modes in which 
    standby D/G system testing may be performed, but does not change the 
    type of testing performed and are not due to modification of the system 
    design. NRC's assessment of the testing of the D/Gs in the 
    configuration proposed is documented in Section 8.3.1, Supplement 1 of 
    the SER (NUREG-0011).
        The proposed amendment does not involve a significant reduction in 
    a margin of safety.
        As previously stated, performance of proposed SRs 4.8.1.1.2.g.1, 
    4.8.1.1.2.g.2, 4.8.1.1.2.g.3, or 4.8.1.1.2.g.4 during Modes 1, 2 or 3 
    will not cause, or result in, an anticipated operational occurrence 
    with attendant challenges to plant safety systems that has not been 
    previously analyzed for the existing monthly surveillances. It also 
    does not change any setpoints or limits established for accident 
    mitigation. Therefore, implementation of the proposed amendment will 
    not reduce the margin of safety for this system.
        Part 3--D/G Steady State Allowable Voltage Range:
        The proposed amendment does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed revisions to the SRs conservatively restrict the 
    allowable range of the D/G steady state voltage. The capability of the 
    D/Gs to provide the required safety function, in support of accident 
    mitigation, will be unaffected or enhanced. Therefore, the proposed 
    revision of the SRs will not increase the consequences of an accident.
        The proposed amendment does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not alter the current functions of the D/
    Gs; therefore, they will not create the possibility of a new or 
    different kind of accident.
        The proposed amendment does not involve a significant reduction in 
    a margin of safety.
        The requirements for emergency D/Gs are unchanged by the 
    conservative revision of the allowable range of the D/G steady state 
    voltage or clarification of the required voltage and frequency after 10 
    seconds. The function of the emergency D/Gs and surveillances to ensure 
    operability will remain the same as currently required by the TS. 
    Therefore, the proposed changes will not result in a reduction in a 
    margin of safety.
    
    [[Page 17237]]
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Project Director: Frederick J. Hebdon.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: February 25, 1998.
        Description of amendment request: Requests Technical Specifications 
    changes to permit use of Option B of 10 CFR 50, Appendix J, for 
    containment leakage testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the KNPP in accordance with the proposed license 
    amendment does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed TS changes do not involve any physical or operational 
    changes to structures, systems or components. The current safety 
    analysis and design basis for the accident mitigation functions of the 
    containment, the airlocks, and the containment isolation valves are 
    maintained. On-site and off-site dose consequences remain unaffected. 
    Containment leakage rate testing is not an accident initiator.
        2. The proposed license amendment request does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The accidents considered are found in the Safety Analysis, Section 
    14 of the USAR. The proposed change does not involve a change to the 
    plant design (structures, systems or components) or operation. No new 
    failure mechanisms beyond those already considered in the current plant 
    Safety Analysis are introduced. No new accident is introduced and no 
    safety-related equipment or safety functions are altered. The proposed 
    change does not affect any of the parameters or conditions that 
    contribute to initiation of any accidents.
        3. The proposed license amendment does not involve a significant 
    reduction in the margin of safety.
        The implementation of Option B potentially affects the frequency of 
    Type A, B, and C containment testing. Except for the determination of 
    test frequency, the methods for performing the actual tests are not 
    changed. NUREG-1493, ``Performance-Based Containment Leak-Test 
    Program'', dated September, 1995, which forms the basis for the 
    Appendix J revision, concludes that adoption of performance-based 
    testing will not significantly reduce the margin of safety. Therefore, 
    the proposed TS amendment will not involve a significant reduction in a 
    margin of safety and will continue to support the design and licensing 
    basis of ensuring an essentially leak-tight containment boundary.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, WI 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P.O. Box 1497, Madison, WI 53701-1497.
        NRC Project Director: Richard P. Savio.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: March 4, 1998.
        Description of amendment request: Requests Technical Specifications 
    changes to provide a one hour Limiting Condition for Operation (LCO) 
    that will permit a safety injection pump to be used for addition of 
    make-up fluid to safety injection accumulators during power operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the KNPP in accordance with the proposed license 
    amendment does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        While filling a safety injection (SI) accumulator, the large break 
    loss of coolant accident (LOCA) would be the bounding accident for pump 
    runout concerns. The proposed LCO would allow relaxation of a single 
    failure being assumed during the short duration of the accumulator 
    fill. The SI pump filling the SI accumulator will be considered to be 
    operable while filling the accumulator.
        Using current KNPP PRA methods, this configuration results in a 
    core damage frequency (CDF) of 5x10-5/year during the five 
    minutes it exists. The increased core damage probability (CDP) due to 
    an accumulator fill is 8x10-11. Conservatively assuming that 
    the accumulator fill occurs every three weeks, the total CDP increase 
    is 1.3x10-9 in a year. The configuration specific DF and CDP 
    increase are well below the limits of 1.0x10-3/year and 
    1.0x10-6, respectively, in the Electric Power Research 
    Institute's PRA Applications Guide. The increase in probability is 
    extremely low and well within industry PRA limits.
        With entry into a one hour action statement, the single failure 
    criterion is relaxed (i.e., a postulated failure of an SI pump is not 
    required) and both SI pumps will provide the required flow to ensure 
    accident mitigation and prevent pump run out. By assuming both SI pumps 
    are available, there is no impact on the accident analysis.
        By remaining within the bounds of the accident analysis and the 
    extremely low increase in the probability of a LOCA concurrent with an 
    accumulator fill, WPSC concludes that this change does not 
    significantly increase the probability or consequences of an accident 
    previously evaluated.
        2. The proposed license amendment requests does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The change allows relaxation of single failure criteria during the 
    short time an SI accumulator would be filled. The SI pump filling the 
    accumulator will be available during the short filling period.
        With entry into a one hour action statement, the single failure 
    criterion is relaxed (i.e., a postulated failure of an SI pump is not 
    required) and both SI pumps will provide the required flow to ensure 
    accident mitigation and prevent pump runout.
        The proposed change is not a result of a hardware change, and with 
    one SI pump considered to be available during an accumulator fill, all 
    the accident analysis requirements are satisfied. Therefore, WPSC 
    concludes that this
    
    [[Page 17238]]
    
    proposed change does not create the possibility of a new or different 
    kind of accident.
        3. The proposed license amendment does not involve a significant 
    reduction in the margin of safety.
        With both SI pumps available during an accumulator fill, there is 
    not an SI pump runout concern and all the requirements of the accident 
    analysis are met. Due to the infrequent occurrence, short duration and 
    extremely low probability of LOCA occurring during an accumulator fill, 
    WPSC concludes there is not significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, WI 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P.O. Box 1497, Madison, WI 53701-1497.
        NRC Project Director: Richard P. Savio.
    
    Previously Published Notices of Consideraton of Issuance of 
    Amendments to Facility Operating Licenses, proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Commonwealth Edison Company, Docket No. 50-237, Dresden Nuclear Power 
    Station, Unit 2, Grundy County, Illinois
    
        Date of amendment request: March 19, 1998.
        Description of amendment request: The proposed amendment would 
    reflect a change in the Dresden, Unit 2, minimum critical power ratio 
    (MCPR) Safety Limit and revise footnotes in Technical Specifications 
    (TS) Section 5.3, to allow the use of Siemens Power Corporation (SPC) 
    ATRIUM-9B fuel.
        Date of publication of individual notice in Federal Register: March 
    26, 1998 (63 FR 14735).
        Expiration date of individual notice: April 27, 1998.
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of amendment request: March 16, 1998.
        Brief description of amendment request: These amendments add a new 
    Limiting Condition for Operation (LCO) 3.0.6 to TS Section 3/4.0, 
    ``APPLICABILITY.'' The new LCO 3.0.6 provides specific guidance for 
    returning equipment to service under administrative control to perform 
    testing required to demonstrate OPERABILITY.
        Date of publication of individual notice in Federal Register: March 
    24, 1998 (63 FR 14142).
        Expiration date of individual notice: Comment period April 7, 1998, 
    and hearing period April 23, 1998.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
    
    Northern States Power Company, Docket No. 50-263, Monticello Nuclear 
    Generating Plant, Wright County, Minnesota
    
        Date of amendment request: March 13, 1998.
        Description of amendment request: The proposed amendment would 
    revise Section 2.1.A of the Technical Specifications (TS) to change the 
    safety limit minimum critical power ratio (SLMCPR) values from 1.08 to 
    1.10 for two recirculation pump operation, and from 1.09 to 1.11 for 
    single loop operation. The amendment would also revise pages 6 and 249b 
    of the TS to indicate that the revised SLMCPR values are applicable 
    only to operating cycle 19.
        Date of individual notice in the Federal Register: March 20, 1998 
    (63 FR 13704).
        Expiration date of individual notice: April 20, 1998.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: March 12, 1998, TXX-98076.
        Description of amendment request: The proposed amendment would 
    provide a temporary Technical Specification change for SRs 
    4.8.1.1.2f.4)b) and 4.8.1.1.2f.6)b) to allow the verification of the 
    auto connected shut-down loads through the load sequencer to be 
    performed at power for fuel cycle 6 on Unit 1 and fuel cycle 4 on Unit 
    2.
        Date of individual notice in the Federal Register: March 27, 1998 
    (63 FR 14974).
        Expiration date of individual notice: April 13, 1998.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Windham County, Vermont
    
        Date of amendment request: March 20, 1997.
        Description of amendment request: The licensee requested to modify 
    their licensing basis by limiting the time the large (18'') purge and 
    vent valves may be open to containment.
        Date of publication of individual notice in Federal Register: March 
    27, 1998. (63 FR 14976).
        Expiration date of individual notice: April 27, 1998.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating
    
    [[Page 17239]]
    
    License, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for A Hearing in connection with these actions was 
    published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendment: December 17, 1997.
        Brief description of amendment: These amendments modify the 
    technical specifications (TS) to remove the reference to Exide 
    batteries with a generic reference to low specific gravity cell 
    batteries.
        Date of issuance: March 16, 1998.
        Effective date: March 16, 1998.
        Amendment No.: Unit 1--116; Unit 2--109; Unit 3--88.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendment revised the Technical Specifications.
        Date of initial notice in Federal Register: January 14, 1998 (63 FR 
    2272).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 16, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of application for amendments: October 22, 1997.
        Brief description of amendments: The amendments change the 
    Technical Specifications (TSs) to incorporate both steady state and 
    transient degraded voltage setpoints as opposed to the current single 
    degraded voltage setpoints. Additionally, the TS decreases the 4 kV 
    voltage range of the emergency diesel generators to assure that the new 
    steady state degraded voltage relays are not actuated during testing.
        Date of issuance: March 17, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 226 and 200.
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 19, 1997 (62 
    FR 61838).
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated March 17, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of application for amendments: November 6, 1997, as 
    supplemented by letters dated January 27, March 3, March 6, March 13, 
    and March 18, 1998.
        Brief Description of amendments: The amendments change the 
    Technical Specifications (TS) for the Brunswick Steam Electric Plant 
    (BSEP) Units 1 and 2 to allow three 18-month diesel generator (DG) 
    surveillance requirements (SR) to be performed during both plant 
    operation (Operational Conditions 1 and 2) and shutdown (Operational 
    Conditions 3, 4, and 5) rather than, as currently required, only during 
    shutdown. The first SR is an inspection of the DG involving a partial 
    disassembly. The second ensures that non-critical DG protective 
    functions are bypassed on an Emergency Core Cooling system actuation 
    signal. The third verifies that the DG operates for greater than or 
    equal to 60 minutes while loaded to at least 3500 kw, which bounds the 
    maximum expected post-accident DG loading. The proposed amendments 
    additionally remove an expired footnote from the BSEP Unit 2 DG TS.
        Date of issuance: March 26, 1998.
        Effective date: March 26, 1998
        Amendment Nos.: 192 and 223.
        Facility Operating License Nos. DPR-71 and DPR-62: Amendments 
    authorize changes to the facility's Technical Specifications.
        Date of initial notice in Federal Register: December 3, 1997 (62 FR 
    63971). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 26, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: April 23, 1997.
        Brief description of amendment: This amendment changes the 
    Technical Specifications Surveillance Requirements for TS 4.3.2.1.1.a, 
    4.3.2.1.4.b, 4.3.2.1.10.a, 4.3.2.1.10.b, and 4.7.3.b.3. to provide more 
    specific information about the tests performed and the components 
    tested.
        Date of issuance: March 18, 1998.
        Effective date: March 18, 1998.
        Amendment No.: 76.
        Facility Operating License No. NPF-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 18, 1997 (62 FR 
    33119).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 18, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County, 
    Michigan
    
        Date of application for amendment: September 29, 1997 (NRC-97-
    0089), as supplemented on March 10, 1998 (NRC-98-0036).
        Brief description of amendment: The amendment revises the technical 
    specifications by relocating the requirements for selected
    
    [[Page 17240]]
    
    instrumentation and the associated Bases from the technical 
    specifications (TS) to the updated final safety analysis report. The 
    affected instrumentation is seismic monitoring (TS 3.7.2), 
    meteorological monitoring (TS 3.7.3), the traversing in-core probe 
    system (TS 3.7.7), the chlorine detection system (TS 3.7.8), and the 
    loose-parts detection system (TS 3.7.10). The TS index and list of 
    tables are also revised to reflect the relocation of these TS and 
    associated Bases. NRC Generic Letter 95-10, ``Relocation of Selected 
    Technical Specification Requirements Related to Instrumentation,'' 
    dated December 15, 1995, provided information concerning relocation of 
    the requirements for these instruments.
        Date of issuance: March 17, 1998.
        Effective date: March 17, 1998, with full implementation within 90 
    days.
        Amendment No.: 115.
        Facility Operating License No. NPF-43: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: October 22, 1997 (62 FR 
    54870). The March 10, 1998, supplement requested a change in the 
    implementation period and was not outside the scope of the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated March 17, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: May 24, 1997.
        Brief description of amendment: The amendment modifies Technical 
    Specification (TS) 3/4.7.4, Ultimate Heat Sink, Table 3.7-3, by 
    incorporating more restrictive dry cooling tower fan requirements, and 
    changes the wet cooling tower water consumption in the TS Bases.
        This amendment modifies the TS to be consistent with revised 
    design-basis calculations.
        Date of issuance: March 23, 1998.
        Effective date: March 23, 1998, to be implemented within 60 days.
        Amendment No.: 139.
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 18, 1997 (62 FR 
    33123).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 23, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station Unit No. 2, Oswego County, New York
    
        Date application for amendment: July 31, 1997.
        Brief description of amendment: This amendment changes Action 
    Statement 36 to TS Table 3.3.3-1, ``Emergency Core Cooling System 
    Actuation Instrumentation,'' to include actions to be taken if more 
    than one channel per trip function should be inoperable in the high-
    pressure core spray drywell pressure and reactor water level 
    instrumentation.
        Date of issuance: March 16, 1998.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 79.
        Facility Operating License No. DPR-63: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 27, 1997 (62 FR 
    45460).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 16, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: October 16, 1996.
        Description of amendment request: The amendment revises the 
    Technical Specifications (TSs) relating to the requirements for AC 
    power sources. The amendment changes certain requirements stated in TS 
    3/4.8.1, ``AC Sources.'' The requirements are related to the emergency 
    diesel generators.
        Date of issuance: March 17, 1998.
        Effective date: As of the date of issuance, with full 
    implementation within 60 days.
        Amendment No.: 54.
        Facility Operating License No. NPF-86: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 18, 1996 (61 
    FR 66711).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 17, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
    
    North Atlantic Energy Service Corporation, et al., Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: February 12, 1997.
        Description of amendment request: The amendment modifies Technical 
    Specification (TS) Section 6.0 ``Administrative Controls,'' to reflect 
    recent organizational changes and changes to the approval title for the 
    Station Qualified Reviewer Program and corrects an incorrect reference 
    in TS 6.4.3.9.b.
        Date of issuance: March 26, 1998.
        Effective date: As of its date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 55.
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 21, 1997 (62 FR 
    27797).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 26, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: July 25, 1997, as supplemented by 
    letters dated November 21, 1997, and March 3, 1998.
        Brief description of amendment: The amendment revises Technical 
    Specifications (TS) 3.5(2), 3.5(3) through 3.5(7), 5.19 and associated 
    Basis to implement Option B of 10 CFR 50 Appendix J.
        Date of issuance: March 23, 1998.
        Effective date: March 23, 1998, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 185.
        Facility Operating License No. DPR-40: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 5, 1997 (62 FR 
    59919).
    
    [[Page 17241]]
    
        The November 21, 1997, and March 3, 1998, supplemental letters 
    provided additional clarifying information that did not change the 
    original no significant hazards determination consideration.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 23, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of application for amendments: February 26, 1997, as 
    supplemented by letters dated December 23, 1997, January 30, 1998, and 
    February 9, 1998.
        Brief description of amendments: The amendments revised the 
    combined Technical Specifications (TS) for the Diablo Canyon Power 
    Plant (DCPP) Unit Nos. 1 and 2 to change TS 3/4.4.5 and 3.4.6.2, 
    including associated Bases 3/4.4.5 and 3/4.4.6.2, to allow the 
    implementation of steam generator (SG) tube voltage based repair 
    criteria for outside diameter stress corrosion cracking (ODSCC) 
    indications at tube-to-tube support plant (TSP) intersections. The 
    allowed primary-to-secondary operational leakage from any one SG would 
    be reduced from 500 gpd to 150 gpd.
        Date of issuance: March 12, 1998.
        Effective date: March 12, 1998, to be implemented within 30 days 
    from the date of issuance.
        Amendment Nos.: Unit 1-124; Unit 2-122.
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 4, 1997 (62 FR 
    17239).
        The December 23, 1997, January 30, 1998, and February 9, 1998, 
    supplemental letters provided additional clarifying information and did 
    not change the staff's initial no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 12, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: March 4, 1997.
        Brief description of amendments: These amendments revise the 
    emergency core cooling system surveillance test acceptance criteria in 
    Technical Specification 3/4.5.2 for the centrifugal charging and safety 
    injection pumps. Specifically, the change would reduce the maximum 
    specified flow rate values for system alignments that affect the 
    suction pressure to the pumps. In the recirculation mode, increased 
    system flow occurs when the charging and safety injection pumps take 
    suction from the discharge of the residual heat removal pumps.
        Date of issuance: March 12, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos: 208 and 189.
        Facility Operating License Nos. DPR-70 and DPR-75: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19834).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 12, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket No. 50-311, Salem Nuclear 
    Generating Station, Unit No. 2, Salem County, New Jersey
    
        Date of application for amendment: October 29, 1997, as 
    supplemented on January 27, 1998.
        Brief description of amendment: The amendment provides a one-time 
    change to Technical Specification 3/4.4.6, ``Steam Generators,'' to 
    require that the next inspection be performed within 24 months from 
    initial criticality for fuel cycle 10, or during the next refueling 
    outage, whichever is first for fuel cycle 10. In addition, the 
    amendment eliminates a description of an alternate steam generator tube 
    sampling plan that was applicable only during the fourth refueling 
    outage.
        Date of issuance: March 19, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No: 190.
        Facility Operating License No. DPR-75: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 17, 1997 (62 
    FR 66142).
        The January 27, 1998, supplemental letter provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 19, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: November 4, 1997.
        Brief description of amendments: These amendments revise the 
    containment systems surveillance test acceptance criteria in Technical 
    Specification 3/4.6.2 for the containment spray pumps. Specifically, 
    the change would replace the Salem Unit 2 minimum specified discharge 
    pressure requirement with an acceptance criterion based on pump 
    differential pressure, and add this surveillance as a new requirement 
    on Salem Unit 1.
        Date of issuance: March 24, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days Amendment Nos.: 209 and 191.
        Facility Operating License Nos. DPR-70 and DPR-75: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 17, 1997 (62 
    FR 66141).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 24, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    South Carolina Electric & Gas Company, South Carolina Public Service 
    Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit 
    No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: February 9, 1998.
        Brief description of amendment: The amendment revises the Virgil C. 
    Summer Nuclear Station Technical Specifications (TS) to remove
    
    [[Page 17242]]
    
    emergency diesel generator (1) accelerated testing requirements (TS 3/
    4.8.1, Table 4.8-1), and (2) special reporting requirements (TS 
    Surveillance Requirement 4.8.1.1.3) in accordance with NRC Generic 
    Letter (GL) 94-01, ``Removal of Accelerated Testing and Special 
    Reporting Requirements for Emergency Diesel Generators.''
        Date of issuance: March 30, 1998.
        Effective date: March 30, 1998.
        Amendment No.: 139.
        Facility Operating License No. NPF-12: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 25, 1998 (63 
    FR 9614) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 30, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: April 24, 1997, as supplemented 
    by letters dated June 6, 1997, and June 27, 1997.
        Brief description of amendment: The amendment revises Section 6.0 
    of the Callaway Plant, Unit 1 Technical Specifications to change the 
    title ``Senior Vice President Nuclear'' to ``Vice President and Chief 
    Nuclear Officer.''
        Date of issuance: March 23, 1998.
        Effective date: March 23, 1998.
        Amendment No.: 122.
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 30, 1997 (62 FR 
    40859).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 23, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Missouri-
    Columbia, Elmer Ellis Library, Columbia, Missouri 65201-5149.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: October 10, 1997, as 
    supplemented on October 31, 1997.
        Brief description of amendment: The amendment revises and clarifies 
    the offsite power requirements.
        Date of Issuance: March 24, 1998.
        Effective date: March 24, 1998, to be implemented within 60 days.
        Amendment No.: 155.
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 31, 1997 (62 
    FR 68319).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated March 24, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of application for amendments: January 21, 1997, as 
    supplemented on December 15, 1997.
        Brief description of amendments: These amendments revise TS Section 
    15.6.11, ``Radiation Protection Program,'' references to Title 10, Code 
    of Federal Regulations, Part 20.
        Date of issuance: March 17, 1998.
        Effective date: March 17, 1998, with full implementation within 45 
    days.
        Amendment Nos.: 182 and 186.
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19837) The December 15, 1997, supplement provided clarifying 
    information and modified proposed language within the scope of the 
    original application and did not change the staff's initial proposed no 
    significant hazards considerations determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 17, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of application for amendments: November 17, 1995 (TSCR 182), 
    as supplemented on July 29, 1996, and December 15, 1997.
        Brief description of amendments: These amendments revise Technical 
    Specifications 15.6.3.2, 15.6.3.3, and 15.6.5 designation of health 
    physics manager to health physicist.
        Date of issuance: March 24, 1998.
        Effective date: March 24, 1998, with full implementation within 45 
    days.
        Amendment Nos.: 183 and 187.
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47983).
        The December 15, 1997, letter provided additional clarifying 
    information within the scope of the original application and did not 
    change the staff's initial proposed no significant hazards 
    considerations determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 24, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
    
        Dated at Rockville, Maryland, this 1st day of April 1998.
    
        For the Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 98-9040 Filed 4-7-98; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
3/16/1998
Published:
04/08/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-9040
Dates:
March 16, 1998.
Pages:
17219-17242 (24 pages)
PDF File:
98-9040.pdf