97-8916. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving no Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 68 (Wednesday, April 9, 1997)]
    [Notices]
    [Pages 17223-17252]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-8916]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving no Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from March 17, 1997 through March 28, 1997. The 
    last biweekly notice was published on March 26, 1997 (62 FR 14457).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed no Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    Involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By May 9, 1997, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert
    
    [[Page 17224]]
    
    opinion which support the contention and on which the petitioner 
    intends to rely in proving the contention at the hearing. The 
    petitioner must also provide references to those specific sources and 
    documents of which the petitioner is aware and on which the petitioner 
    intends to rely to establish those facts or expert opinion. Petitioner 
    must provide sufficient information to show that a genuine dispute 
    exists with the applicant on a material issue of law or fact. 
    Contentions shall be limited to matters within the scope of the 
    amendment under consideration. The contention must be one which, if 
    proven, would entitle the petitioner to relief. A petitioner who fails 
    to file such a supplement which satisfies these requirements with 
    respect to at least one contention will not be permitted to participate 
    as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of amendments request: March 5, 1997.
        Description of amendments request: The proposed amendments would 
    incorporate a new Technical Specification (TS) for instrumentation 
    associated with automatic isolation of a pathway for release of non-
    condensible gases from the main condenser. At power levels of 5 percent 
    or less, mechanical vacuum pumps are used to remove non-condensible 
    gases from the condenser using a pathway to the release stack that 
    bypasses the normal holdup and filter train. The proposed TS will 
    require that four channels of the main steam line radiation--high 
    isolation function be capable of tripping the mechanical vacuum pumps 
    and closing an isolation valve in the release pathway. Surveillance 
    requirements are included in the TS to ensure the isolation 
    instrumentation will perform its intended function.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendments do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change incorporates a new Technical Specification 
    3/4.3.8, ``Condenser Vacuum Pump Isolation Instrumentation.'' This 
    specification will require that the main steam line radiation--high 
    isolation function be capable of tripping the condenser vacuum 
    pump(s) and isolate the associated common isolation valve. Four 
    instrumentation channels of this function are required to be 
    operable when the unit is in OPERATIONAL CONDITION 1 or 2 with a 
    condenser vacuum pump in operation. Adding the requirement to trip 
    the condenser vacuum pumps does not affect the probability of an 
    accident previously evaluated. The probability of component failure 
    of the proposed design for condenser vacuum pump isolation devices 
    is the same as that of the original licensing basis. As a result, 
    the capability to isolate the condenser vacuum pump will not be 
    significantly impacted.
        CP&L contracted Scientech-NUS to recalculate the main control 
    room doses resulting from a control rod drop accident assuming main 
    steam line radiation monitors isolate the condenser vacuum pump(s) 
    and determined the dose to be 23.2 rem thyroid and 0.05 rem whole 
    body, which is less than the General Design Criterion (GDC) 19/
    Standard Review Plan (SRP) Section 6.4 limits of 30 rem thyroid and 
    5 rem whole body. The offsite doses at the exclusion area boundary 
    after 2 hours are 0.16 rem thyroid and 0.015 rem whole body, which 
    is less than the SRP Section 15.4.9 limits. The low population zone 
    (LPZ) dose is estimated to be about 1 rem thyroid, which is also 
    well below regulatory limits. Therefore, the proposed [amendments 
    do] not increase the consequences of an accident previously 
    evaluated.
        2. The proposed amendment[s] would not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        The proposed [amendments add] new requirements to ensure the 
    capability to trip the condenser vacuum pump(s). The proposed 
    [changes do] not affect the operability of equipment designed to 
    mitigate the consequences of an accident nor [do they] create a 
    potential to initiate a new type of accident. Therefore, the 
    proposed [changes do] not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed license [amendments do] not involve a 
    significant reduction in a margin of safety.
        The safety-related main steam line radiation monitors provide a 
    highly reliable means to detect radioactivity resulting from a 
    control rod drop accident and will provide automatic trip of the 
    condenser vacuum pumps and isolation of the associated isolation 
    valve. Use of the main steam line radiation monitors for this 
    application is consistent with the original Brunswick Steam Electric 
    Plant design for condenser pump and associated valve isolation. CP&L 
    contracted Scientech-NUS to recalculate the main control room doses 
    resulting from a control rod drop accident assuming main steam line 
    radiation monitors isolate the condenser
    
    [[Page 17225]]
    
    vacuum pump(s) and determined it to be 23.2 rem thyroid and 0.05 rem 
    whole body, which is less than the GDC 19/SRP Section 6.4 limits of 
    30 rem thyroid and 5 rem whole body. The offsite doses at the 
    exclusion area boundary after 2 hours are 0.16 rem thyroid and 0.015 
    rem whole body, which is less than the SRP Section 15.4.9 limits. 
    LPZ dose is estimated to be about 1 rem thyroid, which is also well 
    below regulatory limits. Therefore, the proposed [changes do] not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: February 18, 1997.
        Description of amendment request: The proposed change revises the 
    Plant System Turbine Cycle Technical Specification (TS) 3/4.7.1 by 
    revising the power range high neutron flux setpoint values in TS Table 
    3.7-1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The high flux setpoints are being revised to provide additional 
    margin against secondary side overpressurization for LOL/TT [loss-
    of-load/turbine trip] events. The proposed revision will not create 
    any loss or reduction in redundancy or diversity in the reactor 
    protection systems that would increase the probability of a 
    previously evaluated accident. The high flux setpoints are being 
    revised to ensure that the consequences of a previously evaluated 
    accident do not increase.
        Therefore, there would be no increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        No new or previously unanticipated failure mechanisms are 
    introduced by the proposed change. No new failure modes have been 
    created by the proposed change. No new credible event or initiating 
    factor is introduced. Reactor power is limited to ensure that the 
    secondary system is not overpressurized.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The margin of safety as defined in the basis of the Technical 
    Specification does not decrease. This change is proposed to ensure 
    that the secondary system pressure will be limited to within 110% of 
    its design pressure during the most severe anticipated operational 
    transient. The revised high flux setpoints are intended to bound the 
    allowable operating configurations of TS Table 3.7-1.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: February 21, 1997.
        Description of amendment request: The proposed change adds a 
    definitive time limit to Technical Specification 3.3.2 in Action 16 of 
    Table 3.3-3 to place an inoperable channel into bypass.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change does not affect the operation or design of 
    the plant in any way. The requirement to place the channel into 
    bypass already exists and this change simply provides a specific 
    time limit. This logic circuit is not an initiator of any event and 
    with no change in logic or operation there is no change in 
    consequences.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed specific time limit does not involve any physical 
    alterations or additions to plant equipment or alter the manner in 
    which any safety-related system performs its function. Therefore, 
    the proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed change replaces an indeterminate time period with a 
    specific limit of six hours. Six hours is a reasonable period in 
    which to complete this requirement and is identical to the time 
    allowed for these functions in NUREG-1431 [Standard Specifications 
    Westinghouse Plants]. Therefore, the proposed change does not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: February 27, 1997.
        Description of amendment request: The proposed change adds sleeve 
    installation as an alternative to tube plugging for repairing degraded 
    steam generator tubes to Technical Specification 3/4.4.5, Steam 
    Generators.
    
    [[Page 17226]]
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The only equipment affected by sleeving is the steam generator 
    tubes. The most severe malfunction of a steam generator tube is a 
    tube rupture. The consequences of a ruptured sleeve are no greater 
    than the consequences of a ruptured tube. Sleeving does not increase 
    the probability of a steam generator tube failure because the 
    sleeved tube has been shown to have a significant safety factor for 
    burst and collapse pressures as well as demonstrated acceptable 
    resistance to corrosion and fatigue loading. Thus, a steam generator 
    with sleeved tubes would perform in the same manner as one without 
    sleeved tubes.
        A sleeved tube is functionally equivalent to an unsleeved tube 
    except for less effective heat transfer due to the air gap and a 
    slightly higher pressure drop due to the primary flow restriction. 
    These differences are bounded by the current tube plugging limits.
        Analysis and testing have demonstrated that the sleeves are 
    structurally adequate to withstand the load existing within the 
    steam generator tubes whether the original tube is still intact or 
    is breeched.
        There is no increase in the possibility for increased fatigue 
    loadings. There is no possibility for the sleeve to become dislodged 
    from its plugging location and enter the RCS [Reactor Coolant 
    System] flow path.
        The plant safety analysis for tube plugging bounds tube 
    sleeving.
        The proposed change has no significant effect on the 
    configuration of the plant. The proposed change does not affect the 
    way in which the plant is operated. Therefore, there would be no 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        A sleeved tube is functionally equivalent to an unsleeved tube 
    except for less effective heat transfer due to the air gap and a 
    slightly higher pressure drop due to the primary flow restriction. 
    These differences are bounded by the current tube plugging limits.
        The sleeved tube has been shown to have a significant safety 
    factor for burst and collapse pressures as well as demonstrated 
    acceptable resistance to corrosion and fatigue loading. Thus, a 
    steam generator with sleeved tubes would perform in the same manner 
    as one without sleeved tubes.
        The proposed change has no significant effect on the 
    configuration of the plant. The proposed change does not affect the 
    way in which the plant is operated. Therefore, the proposed change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed revision to permit the installation of tube sleeves 
    does not reduce the margin of safety as presently defined in 
    Technical Specification BASES section 3/4.4.5. This margin of safety 
    includes primary to secondary leakage limits and tube plugging 
    limits which are not changed by the proposed amendment. The analyses 
    and testing of the proposed sleeve design demonstrates that the 
    structural integrity of the RCS is maintained. Design of the tube 
    sleeve considers mechanical/structural aspects, water chemistry and 
    metallurgical aspects as well as thermal/hydraulic considerations.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: March 10, 1997.
        Description of amendment request: The proposed changes to Technical 
    Specification 3.5.1 provide an optional method of meeting surveillance 
    requirements by allowing the use of instrument readings to meet 
    surveillance 4.5.1.1.a.1, and adds a new Action c to cover a condition 
    in which one accumulator has a boron concentration not within limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The accumulators are not initiators of any event and so the 
    probability of occurrence of an event is unaffected by either of the 
    proposed changes. The use of actual instrumentation readings to 
    comply with the surveillance does not change the function or 
    performance of the accumulators and thus does not affect any 
    accident consequences. The increase in the allowed time to restore 
    the boron concentration to within limits is consistent with allowed 
    out of service times for other Emergency Safeguards equipment.
        It will not have a significant impact on subcriticality during 
    reflood. Therefore, there will be no increase in the consequences of 
    an accident.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the accumulator specification do not 
    involve any physical alterations or additions to plant equipment or 
    alter the manner in which any safety-related system performs its 
    function. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed change to the surveillance requirement provides an 
    equivalent means of meeting the requirement. Since there is no 
    change in either the accumulator limits or the surveillance 
    frequency, there is no reduction in safety margin. The new Action c 
    to address returning the boron concentration of a single accumulator 
    to within limits allows an out of service time commensurate with the 
    times allowed for other Engineered Safeguards Features. The boron 
    concentration of one accumulator does not have a significant impact 
    on subcriticality during reflood and thus does not involve a 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: March 14, 1997.
        Description of amendment request: The amendment will revise the 
    Final Safety Analysis Report to include the
    
    [[Page 17227]]
    
    evaluation of a spent fuel cask drop analysis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The changes described do not impact the probability of 
    occurrence of accidents previously analyzed. Removal of the valve 
    box covers and all but four of the cask closure head sleeve nuts has 
    no impact on accident initiators. Dose assessments using maximum 
    potential releases assuming failure of the spent fuel and 
    radionuclide release through the gap between the cask closure head 
    and the cask or damage to the valves show that no significant 
    increase in consequences of an accident previously evaluated would 
    occur. [Therefore, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.]
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Compromising the integrity of the cask by removing the valve box 
    covers and closure head sleeve nuts in preparation for unloading the 
    spent fuel from the cask does not create the possibility of a new 
    type of accident or equipment malfunction. No safety-related 
    equipment, safety function, or operations of plant equipment will be 
    altered as a result of this change. Therefore, the proposed changes 
    do not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The NRC basis for acceptance of a spent fuel cask drop is 
    documented in Section 15.7.5 of the Safety Evaluation Report, NUREG-
    1038, dated November 1983. It states, ``* * * no loss of cask 
    integrity is postulated to occur in the event of a drop, and the 
    staff concludes there will be no significant radiation released to 
    the environment. The radiological consequences will be less than a 
    small fraction of the 10 CFR 100 exposure guideline values.''
        As described in the proposed change, even though complete cask 
    integrity may not be preserved in the event of a loaded cask drop 
    with the valve box covers removed or with only four, rather than 32, 
    closure head sleeve nuts installed, the radiological consequences 
    calculated using conservative assumptions were determined to be a 
    small fraction of the 10 CFR 100 values. Therefore, the proposed 
    change does not involve a significant reduction in the margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of amendment request: June 20, 1996, as supplemented by 
    letters dated December 30, 1996, and March 5, 1997.
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications (TS) by incorporating NRC approved 
    thermal limit licensing methodology in the list of approved 
    methodologies used in establishing the fuel cycle specific thermal 
    limits. In addition, the proposed amendment would correct mirror 
    editorial items in the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The probability of an evaluated accident is derived from the 
    probabilities of the individual precursors to that accident. The 
    consequences of an evaluated accident are determined by the 
    operability of plant systems designed to mitigate those 
    consequences. Limits will be established consistent with NRC 
    approved methods to ensure that fuel performance during normal, 
    transient and accident conditions is acceptable. The proposed 
    Technical Specifications amendment reflects NRC approved SPC 
    methodology used to analyze normal operations, including anticipated 
    operational occurrences (AOOs), and to determine the potential 
    consequences of accidents.
    
    Licensing Methods and Models
    
        The proposed amendment is to support operation with NRC approved 
    fuel and licensing methods supplied from Siemens Power Corporation 
    [SPC]. In accordance with [Updated Final Safety Analysis Report] 
    UFSAR Chapter 15, the same accidents and transients will be analyzed 
    with the new fuel and methods. The latest NRC approved revision to 
    the Siemens [loss-of-coolant accident] LOCA analysis methodology 
    (Reference: ANF-91-048(P)(A), Advanced Nuclear Fuels Corporation 
    Methodology for Boiling Water Reactors EXEM BWR Evaluation Model) 
    will be used to evaluate the ATRIUM-9B and other co-resident fuel 
    types. The other licensing analysis methods and models are also NRC 
    approved. The approved methods and models are used to determine the 
    fuel thermal limits (e.g., average planar linear heat generation 
    rate, transient linear heat generation rate, minimum critical power 
    ratio and linear heat generation rate). The SPC core monitoring code 
    enables the site to monitor keff as well as control rod density 
    to perform the reactivity anomaly surveillance. Therefore, the 
    change in licensing analysis methods and models does not 
    significantly increase the probability of an accident or the 
    consequences of an accident previously identified. The support 
    systems for minimizing the consequences of transients and accidents 
    are not affected by the proposed amendment.
    
    New Fuel Design
    
        The use of reload quantities of ATRIUM-9B fuel at Dresden does 
    not involve a significant increase in the probability or 
    consequences of any accident previously evaluated in the [Final 
    Safety Analysis Report] FSAR. The ATRIUM-9B fuel is generically 
    approved for use as a reload BWR fuel type (Reference: ANF-89-
    014(P)(A) Revision 1 Supplement 1, Generic Mechanical Design for 
    Advanced Nuclear Fuels 9X9-IX and 9X9-9X BWR Reload Fuel). Limiting 
    postulated occurrences and normal operation have been analyzed using 
    NRC-approved methods for the ATRIUM-9B fuel design to ensure that 
    safety limits are protected and that acceptable transient and 
    accident performance is maintained.
        The reload fuel has no adverse impact on the performance of in-
    core neutron flux instrumentation or CRD response. The ATRIUM-9B 
    fuel design will not adversely affect performance of neutron 
    instrumentation nor will it adversely affect the movement of control 
    blades relative to the current Dresden fuel type, the Siemens 
    manufactured 9x9-2. The exterior dimensions of the ATRIUM-9B fuel 
    have been evaluated by ComEd; the ATRIUM-9B fuel design provides 
    adequate clearances relative to the co-resident 9x9-2 fuel. Thus, no 
    increased interactions with the adjacent control blade or nuclear 
    instrumentation are created. Additionally, given the above mentioned 
    overall envelope similarities, no problems are anticipated with 
    other station equipment such as the fuel storage racks, the new fuel 
    inspection stand and the spent fuel storage pool fuel preparation 
    machine. Therefore, the probability of adverse interactions between 
    the ATRIUM-9B fuel and components in the core and fuel handling 
    equipment is not significantly increased.
        The ATRIUM-9B design is neutronically compatible with the 
    existing fuel types and core components in the Dresden core. SPC 
    tests have demonstrated that the ATRIUM-9B fuel design is 
    hydraulically compatible with the co-resident 9x9-2 fuel. The bundle 
    pressure drop characteristics of the ATRIUM
    
    [[Page 17228]]
    
    9B bundle are similar to those of the 9x9-2 fuel design, hence core 
    thermal-hydraulic stability characteristics are not adversely 
    affected by the ATRIUM-9B design. Cycle stability calculations are 
    performed by SPC. Therefore, the probability of thermal hydraulic 
    instability is not significantly increased.
        Evaluations of the Dresden Emergency Procedures and UFSAR 
    Chapter 15 AOOs are being performed to ensure that the use of the 
    ATRIUM-9B fuel at Dresden does not alter any assumptions previously 
    made in evaluating the radiological consequences of an accident at 
    Dresden Units 2 and 3. Therefore, the radiological consequences of 
    accidents are not significantly increased.
        Methods approved by the NRC are being used in the evaluation of 
    fuel performance during normal and abnormal operating conditions. 
    The ComEd and SPC methods to be used for the cycle specific 
    transient analyses have been previously NRC approved. The proposed 
    methodologies are administrative in nature and do not significantly 
    affect any accident precursors or accident results; as such, the 
    proposed change to the listing of the SPC methodologies for Dresden 
    does not significantly increase the probability or consequences of 
    any previously evaluated accidents.
        The description of the fuel is modified to include the water box 
    design of the NRC approved ATRIUM-9B fuel type.
        Review of the above concludes that the probability of occurrence 
    and the consequences of an accident previously evaluated in the 
    safety analysis report have not been significantly increased.
    * * * * *
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated:
        Creation of the possibility of a new or different kind of 
    accident would require the creation of one or more new precursors of 
    that accident. New accident precursors may be created by 
    modifications of the plant configuration, including changes in 
    allowable modes of operation.
    
    Licensing Methods and Models
    
        The proposed Technical Specification amendment reflects 
    previously approved SPC methodology used to analyze normal 
    operations, including AOOs, and to determine the potential 
    consequences of accidents. In accordance with FSAR Chapter 15, the 
    same accidents and transients will be analyzed with the new fuel and 
    method as have been previously performed. As stated above, the 
    proposed changes do not permit modes of reactor operation which 
    differ from those currently permitted; therefore, the possibility of 
    a new or different kind of accident is not created. Plant support 
    equipment is not affected by the proposed changes; therefore, no new 
    failure modes are created.
    
    New Fuel Design
    
        The basic design concept of a 9x9 fuel pin array with an 
    internal water box has been used in various lead assembly programs 
    and in reload quantities in Europe since 1986. WNP-2 has loaded 
    reload quantities since 1991. Eight lead ATRIUM-9B assemblies were 
    loaded into Dresden 2 during Cycle 15. Approximately 650 water box 
    assemblies have been irradiated in the United States through 1995, 
    with a substantially higher number being irradiated overseas. The 
    NRC has reviewed and approved the ATRIUM-9B fuel design (Reference: 
    ANF-89-014(P)(A) Revision 1 Supplement 1, Generic Mechanical Design 
    for Advanced Nuclear Fuels 9X9-IX and 9X9-9X BWR Reload Fuel). The 
    similarities in fuel design and operation between the ATRIUM-9B and 
    the 9x9-2, and the previous Boiling Water Reactor experience with 
    Siemens fuel, indicate there would be no new or different types of 
    accidents for Dresden than have been considered for the existing 
    fuel. Therefore, the use of ATRIUM-9B fuel at Dresden does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
    * * * * *
        3. Involve a significant reduction in the margin of safety for 
    the following reasons:
        The existing margin to safety is provided by the existing 
    acceptance criteria (e.g., 10 CFR 50.46 limits). The proposed 
    Technical Specification amendment reflects previously approved SPC 
    methodology used to demonstrate that the existing acceptance 
    criteria are satisfied. The revised LOCA methodology has been 
    previously reviewed and approved by the USNRC for application to 
    reload cores of BWRs. References for the Licensing Topical Reports 
    which document this methodology, and include the Safety Evaluation 
    Reports prepared by the USNRC, are added to the Reference section of 
    the Technical Specifications as part of this amendment.
    
    Licensing Methods and Models
    
        The proposed amendment does not involve changes to the existing 
    operability criteria. NRC approved methods and established limits 
    (implemented in the COLR) ensure acceptable margin is maintained. 
    The ComEd and SPC reload methodologies for the ATRIUM-9B reload 
    design are consistent with the Technical Specification Bases. The 
    Limiting Conditions for Operation are taken into consideration while 
    performing the cycle specific and generic reload safety analyses. 
    USNRC approved methods are listed in Specification 6.9.A of the 
    Technical Specifications.
        Analyses performed with USNRC-approved methodology have 
    demonstrated that fuel design and licensing criteria will be met 
    during normal and abnormal operating conditions. The same margins of 
    safety will continue to be utilized by SPC (e.g., limits on peak 
    cladding temperature, cladding oxidation, plastic strain). 
    Therefore, there is not a significant reduction in the margin of 
    safety.
    
    New Fuel Design
    
        The exterior dimensions of the ATRIUM-9B fuel assembly result in 
    equivalent clearances relative to the co-resident 9x9-2 fuel. Thus, 
    no increased interactions with the adjacent control blade and 
    nuclear instrumentation are created. The change does not adversely 
    impact equipment important to safety; therefore the margin of safety 
    is not significantly reduced.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of amendment request: March 18, 1997.
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications (TS) by increasing the High 
    Pressure Coolant Injection (HPCI) isolation setpoint from greater than/
    equal to 80 psig to greater than/equal to 100 psig. The licensee has 
    requested the change to ensure consistency between the Updated Final 
    Safety Analysis Report (UFSAR), design basis documents and the TS. The 
    function of the setpoint is to assure the HPCI turbine steam supply is 
    isolated in the event that the reactor scram supply pressure falls 
    below the stall pressure of the HPCI turbine and the system seals are 
    no longer effective in controlling the release of potentially 
    contaminated steam.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because of the 
    following:
        The Low Reactor Pressure isolation of the HPCI steam supply 
    lines is provided to prevent damage to the HPCI turbine when the 
    reactor steam pressure has decreased below that required to provide 
    adequate motive force to operate the system. The steam supply 
    isolation low reactor pressure setpoint is not an assumed initiator 
    or contributor to any previously evaluated accident and therefore 
    this change does not involve an increase in the probability of an 
    accident previously evaluated at Dresden Station.
        The Lower Reactor Pressure isolation of the HPCI steam supply 
    lines is described in the
    
    [[Page 17229]]
    
    plant safety analysis as a backup protection to other system and 
    facility design features which provide assurance that accident 
    transients will not result in failures of the system which 
    contribute significantly to the consequences of the initiating 
    accident. The low reactor pressure isolation signal provides backup 
    to other isolation signals to ensure isolation will occur, 
    minimizing the radiation dose as a result of steam leakage past the 
    turbine seals in the event of a locked rotor due to damage from 
    liquid carryover due to postulated swell in the reactor vessel.
        These analyses assume the isolation function occurs at 100 psig, 
    and the proposed setpoint of greater than or equal to 100 psig is 
    consistent and conservative with respect to these assumptions. 
    Because the isolation function is not an accident initiator and the 
    revised setpoint ensures that the isolation function continues to 
    minimize radiological consequences, the consequences of any accident 
    previously evaluated is not increased by the proposed changes.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        The proposed change administratively increases the Low Reactor 
    Vessel Pressure trip setpoint which initiates HPCI isolation. This 
    change does not result in any new or different modes of operation. 
    The proposed change increases the setpoint at which the HPCI turbine 
    steam supply will be isolated as the reactor vessel pressure 
    decreases following a postulated accident. The proposed new setpoint 
    is conservative with respect to the existing TS limit, i.e. the new 
    limit of greater than or equal to 100 psig is consistent and 
    permitted by the existing limit of greater than or equal to 80 psig. 
    The change assures that the Trip Setpoint in the TS accurately 
    reflects the design basis and UFSAR described limits.
        Because the proposed change does not result in any new modes of 
    plant operation and administratively increases the system isolation 
    setpoint in a conservative manner, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    those previously evaluated.
        3. Involve a significant reduction in the margin of safety 
    because:
        The Trip Setpoint provides assurance that the HPCI turbine 
    cannot be operated with a steam supply pressure too low to drive the 
    turbine and pump. The isolation assures that the turbine does not 
    stall and minimizes the potential for the release of radioactivity 
    which results from steam leakage past the turbine seals. The 
    proposed change increases the setpoint, ensuring that the required 
    isolation occurs at a higher pressure which is more conservative, 
    i.e. it assures the turbine is isolated before the inlet steam 
    pressure falls to the stall pressure of the HPCI turbine and leakage 
    occurs. The greater than or equal to 100 psig limit is well below 
    the range of reactor vessel pressure for which HPCI is required to 
    perform its safety function. Therefore, the margin of safety 
    provided by the function of the HPCI isolation on low reactor vessel 
    pressure is increased by the proposed TS change, and this change 
    will not involve a reduction in the margin of safety.
        As described, the proposed amendment for Dresden will not reduce 
    the availability of systems required to mitigate accident 
    conditions. Neither are new or significantly different modes of 
    operation proposed. Therefore, the proposed change does not involve 
    a significant reduction in the margin of safety.
        Guidance has been provided in ``Final Procedures and Standards 
    on No Significant Hazards Considerations,'' Final Rule, 51 FR 7744, 
    for the application of standards to license change requests for 
    determination of the existence of significant hazards 
    considerations. This document provides examples of amendments which 
    are and are not considered likely to involve significant hazards 
    considerations.
        This proposed amendment does not involve any irreversible 
    changes, a significant relaxation of the criteria used to establish 
    safety limits, a significant relaxation of the bases for the 
    limiting safety system settings or a significant relaxation of the 
    bases for the limiting conditions for operations. Therefore, based 
    on the guidance provided in the Federal Register and the criteria 
    established in 10 CFR 50.92(c), the proposed change does not 
    constitute a significant hazards consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of amendment request: December 27, 1995, as supplemented 
    September 4, October 18, and November 26, 1996.
        Description of amendment request: The proposed amendment would 
    revise technical specifications (TS) related to electrical power 
    systems. The proposed changes include revisions to limiting conditions 
    for operation (LCO), LCO applicability and action statements, allowed 
    outage times (AOT), surveillance requirements (SR), and administrative 
    controls. The changes add new requirements, revise or delete existing 
    requirements, relocate certain existing requirements to other licensee 
    controlled documents, and editorially restructure the proposed 
    requirements to closely emulate the electrical power system 
    requirements of NUREG-1432, ``Standard Technical Specifications for 
    Combustion Engineering Plants,'' (STS). The proposed requirements 
    differ from the requirements of the STS where necessary to reflect 
    features unique to the Palisades design. Each proposed change has been 
    classified by the licensee as Administrative, Relocated, More 
    Restrictive, or Less Restrictive.
        Basis for proposed no significant hazards consideration 
    determination: A proposed amendment to an operating license for a 
    facility involves no significant hazards consideration if operation of 
    the facility in accordance with the proposed amendment would not: (1) 
    Involve a significant increase in the probability or consequences of an 
    accident previously evaluated; (2) create the possibility of a new or 
    different kind of accident from any previously evaluated; or (3) 
    involve a significant reduction in a margin of safety. As required by 
    10 CFR 50.91(a), the licensee has provided its analysis of the issue of 
    no significant hazards consideration, which is presented below:
    
        Evaluation of ADMINISTRATIVE, RELOCATED, and MORE RESTRICTIVE 
    changes:
        ADMINISTRATIVE changes and RELOCATED changes move requirements, 
    either within the TS or to documents controlled under 10 CFR 50.59, 
    or [clarify] existing TS requirements, without affecting their 
    technical content. Since ADMINISTRATIVE and RELOCATED changes do not 
    alter the technical content of any requirements, they cannot involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated, create the possibility of a new or 
    different kind of accident from any previously evaluated, or involve 
    a significant reduction in a margin of safety.
        MORE RESTRICTIVE changes only add new requirements, or revise 
    existing requirements to result in additional operational 
    restrictions. Since the TS, with all MORE RESTRICTIVE changes 
    incorporated, will still contain all of the requirements which 
    existed prior to the changes; MORE RESTRICTIVE changes cannot 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated, create the possibility of a new or 
    different kind of accident from any previously evaluated, or involve 
    a significant reduction in a margin of safety.
        Evaluation of LESS RESTRICTIVE changes:
        1. Do these LESS RESTRICTIVE changes involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Change 3 revised the requirement for operable AC sources, using 
    more general wording than the existing TS. The existing LCO requires 
    that two explicitly specified transformers be operable; the proposed 
    LCO requires that two qualified offsite circuits be operable. The 
    proposed LCO will allow
    
    [[Page 17230]]
    
    substitution of Safeguards Transformer 1-1 for Station Power 
    Transformer 1-2 as a required AC source, but the quantity and 
    quality of required offsite AC sources is unaffected. Since the 
    capability and qualification of Safeguards Transformer 1-1 are 
    equivalent to those of the Station Power transformer, neither the 
    probability or consequences of an accident previously evaluated will 
    be increased.
        Change 10 is less restrictive only in its allowance of a 72 hour 
    AOT for an inoperable offsite source instead of the 24 hour AOT 
    currently required. The change also makes a considerably more 
    restrictive change by eliminating the allowance, based on submittal 
    of a report, for continuous operation with Startup Transformer 1-2 
    inoperable. Changing an AOT, alone, cannot increase the probability 
    or consequences of an accident previously evaluated.
        Change 14 allows, for an inoperable DG [diesel generator], 
    verification that no common cause failure is involved in lieu of 
    test starting the other DG. The intent of the test starting 
    requirement is to verify that there is no common cause failure which 
    also makes the other DG inoperable. The proposed action statement 
    thereby accomplishes the same objective as that it replaces. Since 
    the proposed action statement accomplishes the same objective as the 
    one it replaces, operation in accordance with the proposed change 
    will not increase the probability or consequences of an accident 
    previously evaluated.
        Change 21 revises the SR for the DG starting test. [The ``Less 
    Restrictive'' elements of the change eliminate the requirement to 
    vary use of the A and B starting circuits for each monthly test, 
    because the DG is not assumed to be single failure proof; and 
    eliminate requirements that the DGs be manually started and that 
    they be synchronized from the control room, because no practical 
    alternatives exist for accomplishing these actions]. The proposed 
    change does not alter any plant operating conditions, operating 
    practices, equipment settings, or equipment capabilities. Therefore, 
    operation of the facility in accordance with the proposed change 
    will not involve an increase in the probability of an accident. 
    Change 21 requires more rigorous testing of the DGs than required by 
    the existing Technical Specifications. The more rigorous testing is 
    intended to provide additional assurance that the DGs are capable of 
    performing their design function and should, therefore, involve a 
    reduction, rather than an increase, in the consequences of those 
    accidents previously evaluated.
        Change 25 revises the SR for testing the fuel transfer system. 
    The proposed change does not alter any plant operating conditions, 
    operating practices, equipment settings, or equipment capabilities. 
    Therefore, operation of the facility in accordance with the proposed 
    change will not involve an increase in the probability of an 
    accident. The only ``Less Restrictive'' feature of proposed SR is 
    test interval extension from ``each month'' to ``each 92 days.'' 
    Changing a surveillance frequency, alone, cannot increase the 
    probability or consequences of an accident previously evaluated.
        Change 26 revises the station battery SRs. The proposed monthly 
    and quarterly battery SRs contain all of the test requirements of 
    the existing SRs with two exceptions: (1) The proposed interval for 
    measuring each cell voltage is ``each 92 days'' instead of the 
    existing ``every month'' and (2) the requirement to record the 
    amount of water added has been deleted. Changing a surveillance 
    frequency or deleting a maintenance record cannot increase the 
    probability or consequences of an accident previously evaluated.
        2. Do changes create the possibility of a new or different kind 
    of accident from any previously evaluated?
        Change 3 only involves the specified offsite power sources. 
    Since the Loss of Offsite Power is already considered in the 
    accident analyses, operating the facility in accordance with Change 
    3 will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        Change 10 revises an AOT; Change 14 revises a required action; 
    Change 21 revises a testing requirement; Changes 25 and 26 revise a 
    surveillance interval; and Change 26 deletes the requirement for a 
    maintenance record. None of these proposed changes alter any plant 
    operating conditions, operating practices, equipment settings, or 
    equipment capabilities. Therefore, operation of the facility in 
    accordance with the proposed changes will not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. Do changes involve a significant reduction in a margin of 
    safety?
        Change 3 does not alter the quantity or quality of offsite 
    sources required to be available. Therefore, operating the facility 
    in accordance with the proposed change will not involve a reduction 
    in a margin of safety.
        Change 10 revises an AOT; Change 14 revises a required action, 
    Change 21 revises a testing requirement; Changes 25 and 26 revise a 
    surveillance interval; and Change 26 deletes the requirement for a 
    maintenance record. These proposed changes do not alter any plant 
    operating conditions, operating practices, equipment settings, or 
    equipment capabilities. Therefore, operating the facility in 
    accordance with the proposed change will not involve a reduction in 
    a margin of safety.
    
        The licensee's September 4, 1996, supplement stated that three of 
    the proposed changes contained in the supplement were not addressed in 
    the December 27, 1995, no significant hazards analysis. The changes 
    involved TS requirements that would be deleted. Equivalent requirements 
    would be incorporated in the FSAR or other documents subject to the 
    controls of 10 CFR 50.59. The licensee's analysis of the issue of no 
    significant hazards consideration for these changes is presented below:
    
        1. Do changes which relocate a requirement from the TS to 
    documents which are controlled under 10 CFR 50.59 involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated?
        10 CFR 50.59 specifically prohibits [without obtaining prior NRC 
    review and approval] changes to the facility as described in the 
    safety analysis report, and to procedures described in the safety 
    analysis report ``if the probability of occurrence or the 
    consequences of an accident or malfunction of equipment important to 
    safety previously evaluated in the safety analysis report may be 
    increased''. Since the conditions which limit changes performed 
    under 50.59 are more restrictive than the conditions which define 
    changes considered to involve a significant hazards consideration, 
    relocation of a requirement from the TS to the FSAR [Final Safety 
    Analysis Report] or to documents which are referenced by the FSAR 
    cannot involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Do changes which relocate a requirement from the TS to 
    documents which are controlled under 10 CFR 50.59 create the 
    possibility of a new or different kind of accident from any 
    previously evaluated?
        10 CFR 50.59 specifically prohibits [without obtaining prior NRC 
    review and approval] changes to the facility as described in the 
    safety analysis report, and to procedures described in the safety 
    analysis report ``if a possibility for an accident or malfunction of 
    a different type than any evaluated previously in the safety 
    analysis report may be created''. Since the conditions which limit 
    changes performed under 50.59 are more restrictive than the 
    conditions which define changes considered to involve a significant 
    hazards consideration, relocation of a requirement from the TS to 
    the FSAR or to documents which are referenced by the FSAR cannot 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. Do these changes which relocate a requirement from the TS to 
    documents which are controlled under 10 CFR 50.59 involve a 
    significant reduction in a margin of safety?
        10 CFR 50.59 specifically prohibits [without obtaining prior NRC 
    review and approval] changes to the facility as described in the 
    safety analysis report, and to procedures described in the safety 
    analysis report ``if the margin of safety as defined in the basis 
    for any technical specification is reduced''. Since the conditions 
    which limit changes performed under 50.59 are more restrictive than 
    the conditions which define changes considered to involve a 
    significant hazards consideration, relocation of a requirement from 
    the TS to the FSAR or to documents which are referenced by the FSAR 
    cannot involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analyses and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
    
    [[Page 17231]]
    
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: John N. Hannon.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: March 10, 1997.
        Description of amendment request: The proposed amendment would 
    modify Unit 1 Technical Specification (TS) 5.2.1 to add ZIRLO as fuel 
    assembly material and add reference to Nuclear Regulatory Commission 
    approved Topical Report, WCAP-12610, ``Vantage+ Fuel Assembly Reference 
    Core Report'', to TS 6.9.1.12 for both units.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The methodologies used in the accident analyses have been 
    modified to reflect the requirements provided in WCAP-12610, 
    VANTAGE+ Fuel Assembly Reference Core Report. Reference to this NRC 
    approved ZIRLO topical report has been added to Specification 
    6.9.1.12, for both units to ensure the analytical methods used to 
    determine the core operating limits are consistent with those 
    previously approved by the NRC. The proposed changes do not change 
    or alter the design assumptions for the systems or components used 
    to mitigate the consequences of an accident. Use of ZIRLO fuel rod 
    material does not adversely affect fuel performance or impact 
    nuclear design methodology. Therefore, accident analysis results are 
    not impacted.
        The operating limits will not be changed and the analysis 
    methods to demonstrate operation within the limits will remain in 
    accordance with NRC approved methodologies. Other than the changes 
    to the fuel assemblies, there are no physical changes to the plant 
    associated with this technical specification change. A safety 
    analysis will continue to be performed for each cycle to demonstrate 
    compliance with all fuel safety design bases.
        VANTAGE 5H fuel assemblies with ZIRLO fuel rods meet the same 
    fuel assembly and fuel rod design bases as other VANTAGE 5H fuel 
    assemblies. In addition, the 10 CFR 50.46 criteria are applied to 
    the ZIRLO fuel rods. The use of these fuel assemblies will not 
    result in a change to the reload design and safety analysis limits. 
    Since the original design criteria are met, the ZIRLO fuel rods will 
    not be an initiator for any new accident. The fuel rod material is 
    similar in chemical composition and has similar physical and 
    mechanical properties as Zircaloy-4. Thus, the fuel rod integrity is 
    maintained and the structural integrity of the fuel assembly is not 
    affected. ZIRLO improves corrosion performance and dimensional 
    stability. No concerns have been identified with respect to the use 
    of an assembly containing a combination of Zircaloy-4 and ZIRLO fuel 
    rods.
        The dose predictions in the safety analyses are not sensitive to 
    the fuel rod material used; therefore, the radiological consequences 
    of accidents previously evaluated in the safety analysis remain 
    valid. A reload analysis is completed for each cycle, in accordance 
    with NRC approved methodologies. Therefore, the proposed change does 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        VANTAGE 5H fuel assemblies with ZIRLO fuel rods satisfy the same 
    design bases as those used for other VANTAGE 5H fuel assemblies. All 
    design and performance criteria continue to be met and no new 
    failure mechanisms have been identified. The ZIRLO fuel rod material 
    offers improved corrosion resistance and structural integrity.
        The proposed changes do not affect the design or operation of 
    any system or component in the plant. The safety functions of the 
    related structures, systems, or components are not changed in any 
    manner, nor is the reliability of any structure, system, or 
    component reduced. The changes do not affect the manner by which the 
    facility is operated and do not change any facility design feature, 
    structure, or system. No new or different type of equipment will be 
    installed. Since there is no change to the facility or operating 
    procedures, and the safety functions and reliability of structures, 
    systems, or components are not affected, the proposed changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The use of Zircaloy-4, ZIRLO, or stainless steel filler rods in 
    fuel assemblies will not involve a significant reduction in the 
    margin of safety because analyses using NRC approved methodology 
    will be performed for each configuration to demonstrate continued 
    operation within the limits that assure acceptable plant response to 
    accidents and transients. These analyses will be performed using NRC 
    approved methods that have been approved for application to the fuel 
    configuration.
        Use of ZIRLO as fuel rod material does not change the VANTAGE 5H 
    reload design and safety analysis limits. The use of these fuel 
    assemblies will take into consideration the normal core operating 
    conditions allowed in the technical specifications. For each reload 
    core, the fuel assemblies will be evaluated using NRC approved 
    reload design methods, including consideration of the core physics 
    analysis peaking factors and core average linear heat rate effects.
        Based on the above, it is concluded that the proposed license 
    amendment request does not result in a significant reduction in 
    margin with respect to plant safety as defined in the UFSAR [Updated 
    Final Safety Analysis Report] or any plant technical specification 
    BASES.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: July 17, 1996.
        Description of amendment request: The proposed amendment would 
    reflect that the name of Louisiana Power & Light Company, which is 
    licensed to own and possess Waterford 3, has been changed to Entergy 
    Louisiana, Inc.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No
        The proposed change documents changing the legal name of the 
    company. The proposed change will not affect any other obligations. 
    The company will still own all of the same assets, they still serve 
    the same customers, and all existing obligations and commitments 
    will continue to be honored. Therefore, the proposed change will not 
    involve a significant increase in the probability or consequences of 
    any accident previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No
        The administrative changes in the Operating License requirements 
    do not involve any change in the design of the plant. Therefore, the 
    proposed change will not create the possibility of a new or 
    different
    
    [[Page 17232]]
    
    kind of accident from any accident previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No
        The proposed change is administrative in nature and does not 
    reduce the level of safety imposed by any current requirement. 
    Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: October 16, 1996.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) action requirements 3.2.1 and 3.2.4 
    and their associated surveillance requirements to extend the allowable 
    time for the Core Operation Limit Supervisory System (COLSS) to be out 
    of service by monitoring for adverse trends in the linear heat rate 
    (LHR) and departure from nucleate boiling (DNBR) limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No
        The proposed change does not modify the requirement to operate 
    within the alternate LHR and DNBR limits nor does it modify the 
    actual LHR or DNBR limits themselves. In the case of exceeding a 
    COLSS calculated [power operating limit] POL, Entergy agrees that 
    corrective action should be initiated promptly to bring the LHR and 
    DNBR within their respective limits and, in this case, a 15 minute 
    time limit is appropriate. However, in the case of exceeding a [core 
    protection calculator] CPC calculated operating limit following the 
    loss of COLSS, it is clear that simply because COLSS execution was 
    lost does not mean that the plant is operating outside the range of 
    conditions assumed in the Chapter 15 Safety Analysis and, in this 
    case, a 15 minute time limit is not appropriate. An increase from 2 
    hours to 8 hours to regain the monitoring capabilities of COLSS 
    would not significantly increase the probability of exceeding the 
    actual LHR or DNBR power operating limits since the increase in 
    COLSS out-of-service time will be compensated for by monitoring for 
    adverse trends of the important CPC calculated parameters (DNBR 
    Margin and LHR). Further, since the proposed change will result in 
    maintaining steady-state conditions while monitoring for adverse 
    trends, it will be easier for the operators to detect any abnormal 
    occurrence that has the potential to degrade either the LHR or the 
    DNBR.
        The primary consideration in extending the COLSS out of service 
    time limit is the remote possibility of a slow, undetectable 
    transient that degrades the LHR and/or DNBR slowly over the 8 hour 
    period and is then followed by an [anticipated operational 
    occurrence] AOO or an accident. The parameters normally monitored by 
    COLSS which have the potential for degrading the LHR and DNBR if no 
    corrective action is taken are: Reactor Coolant System (RCS) flow 
    rate, axial and radial power distributions, core inlet temperature, 
    core power, RCS pressure and azimuthal tilt. Of these parameters, 
    core inlet temperature, core power, and RCS pressure are easily 
    monitored by the plant operators using various safety-grade, 
    Redundant Control Room indications and, therefore, changes in these 
    parameters are readily apparent. Further, operating experience at 
    Waterford 3 and other [Combustion Engineering] CE nuclear steam 
    supply systems using the same reactor coolant pumps (RCPs) as 
    Waterford has shown that measurable changes in RCP Ps 
    (which COLSS uses to calculate RCS flow) are very rare and when they 
    do occur, involve abrupt step changes in flow which are readily 
    apparent; hence, the probability of a slow degradation in the RCS 
    flow rate is exceedingly small. Thus, the parameters that 
    comparatively (although still remote) pose the most potential for a 
    degradation in the core thermal margin when COLSS is out of service 
    relate to the axial and radial core power distributions and the 
    azimuthal tilt. These parameters are discussed below.
        Axial xenon oscillations are a normal consequence of the 
    Waterford 3 core design, particularly near the end of core life. As 
    a result, Waterford 3 operations personnel are instructed, per 
    operating procedure OP-10-001, General Plant Operations, to maintain 
    strict control over the axial power shape in the core. Although the 
    primary reason for axial shape control is to maintain an even fuel 
    burnup throughout the core, it also results in maintaining the axial 
    power shapes well within the limits assumed in the safety analysis. 
    Typically, axial shape control practiced at Waterford 3 maintains 
    the axial shape index (ASI) within 0.05 ASI units of the equilibrium 
    shape index (ESI), which is normally very near 0.0.
        Hypothetically, the most severe situation which could be 
    postulated to occur, although again remote, would be if COLSS 
    execution was lost just when the plant operators were ready to take 
    manual action to return the ASI value to within the ESI + 0.05 
    control band. Since a full xenon oscillation takes approximately 26 
    hours, there would be about 6 hours from the time that control 
    action would normally be taken to the time that the ASI reached its 
    peak value (i.e., it takes one quarter cycle for the ASI to travel 
    from its ESI value to its peak value). Since abnormal operating 
    procedure OP-901-501, PMC or Core Operating Limit Supervisory System 
    Inoperable, will be revised to require the CPC calculated LHR and 
    DNBR trends to be monitored every 15 minutes (see below), any 
    significant change in the axial shape index will be apparent through 
    a change in these CPC calculated values. Hence, due to the attention 
    given the axial power distribution, both when COLSS is in service as 
    well as when COLSS is out of service it is very improbable that a 
    change in ASI during eight hours of steady-state operation with 
    COLSS out of service could be either undetected or lead to a 
    condition that placed the reactor outside the range of initial 
    conditions that were assumed in the safety analysis.
        With regards to azimuthal tilt, there is very rarely any 
    significant change in this parameter as long as all [control element 
    assembly] CEAs are properly aligned. The only real contributor to a 
    rapid increase in azimuthal tilt would be an inadvertent CEA drop; 
    however, since the probability of a CEA drop is very low, the 
    likelihood of this event occurring within the eight hour time limit 
    is even lower. In the unlikely event that a CEA drop did occur, the 
    Control Element Assembly Calculators (CEACs) provide a safety-grade, 
    redundant means of alerting the operators that corrective action is 
    necessary. Thus, the potential for a degradation in azimuthal tilt 
    during eight hours of steady-state operation following the loss of 
    COLSS is both highly unlikely and relatively easy to detect using 
    instrumentation already available in the Control Room.
        As previously stated, upon approval of the proposed change plant 
    personnel will revise abnormal operating OP-901-501, PMC or Core 
    Operating Limit Supervisory System Inoperable, to monitor for 
    adverse trends of the CPC calculated values of LHR and DNBR. 
    Currently, this procedure requires that the monitoring frequency for 
    LHR and DNBR be increased to once every 15 minutes on a loss of 
    COLSS.
        Extending the time to restore the CPC calculated LHR and DNBR to 
    within the acceptable operating range from 2 hours to 8 hours is 
    being proposed to assure that COLSS can be restored thus decreasing 
    the probability of an avoidable challenge to the reactor protection 
    system (RPS) during a power reduction. It is possible that the 
    required power reductions may exceed 25% near the end of the fuel 
    cycle. These large power reductions result in a rapid increase in 
    xenon concentration, changes in ASI, and a subsequent decrease in 
    cold leg temperature (T-cold) that may be difficult to control. 
    Accordingly, given the potential for
    
    [[Page 17233]]
    
    power reductions of this magnitude, it is appropriate to extend the 
    time allowed to restore COLSS so that a power reduction may be 
    unnecessary.
        Taken in total, the proposed changes will reduce the number of 
    potentially unnecessary power reductions by allowing more time for 
    COLSS to be restored along with the advantages of trend monitoring 
    in detecting an adverse trend expeditiously. The proposed change 
    will result in significant operational benefits while continuing to 
    maintain a high degree of confidence that the core conditions remain 
    well within the range of values assumed in the safety analysis.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No
        The proposed change does not alter the current power operating 
    limits nor does it involve any changes to COLSS or CPC software. 
    There has been no physical change to plant systems, structures or 
    components nor will the proposed change affect the ability of any of 
    the safety-related equipment required to mitigate AOOs or accidents. 
    The only significant change associated with the proposed amendment 
    involves changes to the operating procedures used when COLSS is out-
    of-service. All revisions to operating procedures will be reviewed 
    and approved by appropriate plant personnel as required by the 
    Administrative Controls (Section 6) in the Waterford 3 Technical 
    Specifications. Therefore, the proposed change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No
        The intent of [limiting conditions for operation] LCOs 3.2.1 and 
    3.2.4 is to maintain the reactor within the range of initial 
    conditions that was assumed in the Safety Analysis. Maintaining the 
    LHR within the specified range ensures that in the event of a LOCA, 
    the fuel cladding temperature will not exceed the 2200 deg.F limit 
    imposed by 10CFR46 [10 CFR Part 46]. Maintaining the DNBR within the 
    specified range ensures that no AOO will result in a violation of 
    the [Specified Acceptable Fuel Design Limits] SAFDLs and that no 
    postulated accident will result in consequences more severe than 
    those described in Chapter 15 of the [Final Safety Analysis Report] 
    FSAR. Since there has been no change to the requirement to operate 
    the reactor within the LHR and DNBR limits and no change to the 
    actual LHR and DNBR limits themselves, the accident analyses 
    described in Chapter 15 of the FSAR will not be affected and will 
    therefore remain bounding.
        The proposed change will reduce the number of potentially 
    unnecessary power reductions along with the rate at which the power 
    reductions are accomplished. Maintaining steady-state conditions for 
    up to eight hours after the loss of COLSS while monitoring the CPC 
    LHR/DNBR for trends, provides plant personnel with a reasonable 
    period of time to return COLSS to service while continuing to 
    maintain a high degree of confidence that the core conditions remain 
    well within the range of values assumed in the safety analysis. In 
    fact, monitoring for trends in LHR and DNBR Margin increases the 
    margin of safety by allowing the anticipation of degradation in LHR 
    or DNBR Margin. Moreover, by reducing the number of plant transients 
    there will be an attendant reduction in probability of an AOO and 
    subsequent RPS actuation. Therefore, the proposed change will not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn, 1400 
    L Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: October 16, 1996.
        Description of amendment request: The following changes to the 
    Waterford Steam Electric Station, Unit 3, Technical Specifications are 
    proposed: 1) Relocation of certain administrative controls to the 
    Quality Assurance Program Manual (QAPM) as described in Nuclear 
    Regulatory Commission Administrative Letter 95-06, ``Relocation of 
    Technical Administrative Controls related to Quality Assurance''; 2) 
    Change shift coverage from 8-hour day, 40-hour weeks to an option of 8 
    or 12 hour days and nominal 40-hour weeks; 3) Make certain editorial 
    changes to the titles of certain organizational positions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No
        The conditions as they exist in the present Technical 
    Specifications do not have an affect on either the probability or 
    consequences of a previously evaluated accident. These changes also 
    will have no impact to increase either the probability or 
    consequences of a previously evaluated accident.
        The proposed changes will have no affect on design basis 
    accidents nor will the change directly affect any material condition 
    of the plant that could directly contribute to causing or mitigating 
    the effects of an accident.
        Therefore, the proposed changes will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No
        The proposed changes will not alter the operation of the plant 
    or the manner in which it is operated. The changes do not involve a 
    design change and do not introduce any new failure modes.
        Therefore, the proposed changes will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in margin of safety?
        Response: No
        The proposed changes are administrative in nature and affect 
    only Section 6.0 of the Technical Specifications. The Waterford 3 
    margins of safety are defined in Sections 2 through 5 and are 
    unaffected by these changes. Moving the reviews from the TS to the 
    QAPM will have no affect on the margin of safety because reviews 
    will still be performed. The only difference is the reviews will be 
    administratively controlled by the QAPM. The QAPM is controlled by 
    10CFR50.54 so no changes can be made which would lessen these 
    commitments (i.e., remove or reduce the requirement for procedure 
    reviews) without prior NRC approval.
        Changing from an 8 hour to an 8 or 12 hour shift will not have 
    an adverse impact on personnel performance. The NRC study documented 
    in NUREG CR-4248 has identified that personnel errors have decreased 
    and productivity has increased where this change has been 
    implemented.
        Therefore, the proposed changes will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans
    
    [[Page 17234]]
    
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: March 27, 1997.
        Description of amendment request: The proposed change modifies 
    Technical Specification 3/4.5.2, ``ECCS Subsystems Modes 1, 2, and 3.'' 
    The proposed change adds a surveillance requirement to verify the 
    Emergency Core Cooling System (ECCS) piping is full of water at least 
    once per 31 days. A change to the Technical Specification Basis 3/4.5.2 
    and 3/4.5.3 has been included to support this change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The proposed change will not affect the assumptions, design 
    parameters, or results of any accident previously evaluated. The 
    proposed change does not add or modify any existing equipment. The 
    proposed change adds a new surveillance requirement which will 
    minimize the likelihood of a pressure transient occurring during 
    system startup and provide increased assurance that the ECCS will 
    perform its design basis function when needed. The new [low pressure 
    safety injection] LPSI and [high pressure safety injection] HPSI 
    vent valves which may be manipulated during this surveillance will 
    be administratively controlled and will be locked close when not in 
    use to prevent the possibility of a flow diversion. This 
    surveillance requirement is consistent with NUREG 1432.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        While new vent lines are being installed under 10CFR50.59, this 
    proposed change adds only a new surveillance requirement to 
    Technical Specification 3/4.5.2 and therefore does not involve 
    modifications to any existing equipment. The new vent valves, when 
    required, will be operated and controlled in the same manner as 
    existing LPSI and HPSI vent valves. The new LPSI and HPSI vent 
    valves will be administratively controlled and will be locked close 
    when not in use. This surveillance requirement is consistent with 
    NUREG 1432.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        The functionality of ECCS is maintained such that it is capable 
    of performing its design function as assumed in the Updated Final 
    Safety Analysis Report. Verifying the ECCS is full of water at least 
    once per 31 days will minimize the likelihood of a pressure 
    transient occurring during system startup and provide increased 
    assurance that the ECCS will perform its design basis function when 
    needed. This surveillance requirement is consistent with NUREG 1432.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: March 27, 1997.
        Description of amendment request: The proposed change modifies 
    Technical Specification (TS) surveillance requirements 4.5.2.d.3 and 
    4.5.2.d.4. The proposed change specifies granular trisodium phosphate 
    dodecahydrate (TSP), increases the minimum required amount of TSP that 
    is maintained in containment during power operation, and adjusts the 
    TSP sampling requirement accordingly. A change to the TS Basis 3/4.5.2 
    has been included to support this change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        Granular trisodium phosphate dodecahydrate is stored in the 
    containment lower level to raise the pH of the sump and spray water 
    following a LOCA. As the pH of the water increases, more radioactive 
    iodine is kept in solution and the amount of airborne radioactive 
    leakage is decreased. This also lessens the potential for boric acid 
    solution reacting with galvanized metal in containment to release 
    hydrogen. An additional advantage of a higher pH is the beneficial 
    reduction in chloride stress corrosion cracking of metal components 
    in the containment following an accident.
        This chemical is an accident mitigator, not an accident 
    initiator in that it is not used until after an accident has 
    occurred. At the time it goes into solution, the accident has 
    occurred, containment spray has been activated and water has 
    collected in the sump. Therefore, increasing the Technical 
    Specification minimum amount verified to be in containment or 
    changing the sample solution and sample size will not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        At the time TSP goes into solution, the accident has occurred, 
    containment spray has been activated and water has collected in the 
    containment sump. At Waterford 3, the iodine partition factor is a 
    constant 50% and does not vary with pH as allowed in the Standard 
    Review Plan (SRP) revision 1. The curve in SRP 6.5.2 revision 1 
    allows a partition factor of at least 50% for containment water at a 
    pH of 6.5 or less. The partition factor increases as pH rises. But, 
    the curve is based on sodium hydroxide which is much more reactive 
    than TSP. Therefore, increasing the Technical Specification minimum 
    amount verified to be in the containment, and corresponding sample 
    size, will not involve any significant increase in the consequences 
    probability of an accident because no credit is taken for reducing 
    the amount of volatized iodine normally associated with a 7.0 pH 
    solution.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        The addition of more TSP does not represent a significant change 
    in the configuration or operation of the plant. Trisodium phosphate 
    dodecahydrate is currently present in the containment lower level. 
    Design Change 3491 which increases the storage capacity of the TSP 
    storage baskets was evaluated in accordance with 10 CFR 50.59 and 
    found not to involve an unreviewed safety question.
    
    [[Page 17235]]
    
        Boric acid acts as a buffer to prevent the pH from rising above 
    approximately 8.1 as TSP is dissolved. An internal study (EC-S96-013 
    revision 0) has shown that given the ``ratio of grams of TSP to 
    liters of 3000 ppm boron solution'' stays less than 5.6, TSP cannot 
    increase pH above 8.2. As pH increases, components composed of 
    aluminum, zinc, or copper become vulnerable to corrosion. Branch 
    Technical Position MTEB 6-1 implies that a solution pH greater than 
    7.5 enhances the chance for hydrogen generation as a result of 
    aluminum corrosion. Waterford 3 administratively limits the amount 
    of aluminum in containment to minimize the amount of hydrogen 
    expected during a DBA. Zinc is a component of the paint applied to 
    surfaces inside containment. The hydrogen recombiner design basis 
    includes 464 square feet (1040 pounds) of aluminum and 419,300 
    square feet (17,252 pounds) of metallic zinc. Estimates of the 
    amount of hydrogen produced by the aluminum assumes that the 
    corrosive agent is sodium hydroxide--a much more active chemical 
    than is TSP. Thus, the amount of hydrogen expected in the FSAR for 
    the hydrogen recombiner bounds what would actually be produced by 
    TSP even at a pH of approximately 8.1.
        The 4.5.2.d.3 proposed TSP to boron ratio assures that pH cannot 
    rise above 8.1 as long as post accident in-containment boric acid 
    solution concentration is no greater than 3011 ppm boron and no less 
    than 1504 ppm boron. The main variable in post accident 
    concentration (the difference between 1504 and 3011) is the 
    concentration in the RCS at the time of the accident.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        Trisodium phosphate dodecahydrate is stored in the containment 
    lower level to raise the pH of the sump and spray water following a 
    LOCA. As the pH of the water increases, more radioactive iodine is 
    kept in solution and the amount of airborne radioactive leakage is 
    decreased. A neutral pH also reduces the hydrogen generation from 
    the corrosion of the galvanized materials in containment. An 
    additional advantage of a higher pH is the beneficial reduction in 
    chloride stress corrosion cracking of metal components in the 
    containment following an accident.
        Technical Specification 4.5.2.d.3 requires verification that a 
    minimum volume of TSP is contained in the storage baskets in 
    containment. Nine previous runs of surveillance requirement 
    4.5.2.d.4 (and similar tests) showed that the TSP actually used in 
    the plant properly neutralized a sample of water borated within RWSP 
    boron concentration limits. Boron concentrations of eight of the 
    sample solutions used in these tests ranged from 1753 ppm to 2217 
    ppm and resulted in a pH of 7.02 or greater. (The boron 
    concentration of one test performed in 1986 was unavailable.) The 
    ratio 4 grams to 4 liters is the amount of TSP needed to bring the 
    solution to a pH of at least 7.0 given that the solution is in the 
    1753 to 2217 ppm Boron range.
        The amount of TSP in containment currently is adequate assuming 
    that RCS boric acid concentration stays below 454 ppm. However, the 
    fuel cycle is nearly over and a restart with a refreshed core would 
    require substantially more boric acid. We expect that the 
    containment water would reach approximately 2400 ppm under ideal 
    circumstances during cycle 9. During cycle 10, boron concentration 
    in containment could reach 3011 under those same ideal conditions. 
    As the maximum boron concentration increases, there is a non-linear 
    increase in the amount of TSP needed to raise solution pH to 7.0. 
    Thus, we request that the minimum amount of TSP in containment 
    required by 4.5.2.d.3 to be increased from 97.5 cubic feet to 380 
    cubic feet. This change also proposes to adjust the 4.5.2.d.4 
    specified increase that sample solution and the TSP sample size 
    accordingly. This change will ensure the safety injection 
    containment sump, when filled with water, will have an acceptable pH 
    following a LOCA. The test will not only demonstrate that TSP is in 
    the baskets but also shows that the amount of TSP in containment can 
    neutralize the solution expected in containment during any DBA.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety. The amount of iodine kept in 
    solution during a DBA is limited to 50%. Note, the pH scale is 
    logarithmic so that the amount of TSP needed to raise pH to 7.0 is 
    more than three times the amount needed to reach 6.5. Furthermore, 
    the amount of hydrogen generated during a DBA is over estimated by 
    the analysis when it used sodium hydroxide as the corrosive agent 
    rather than TSP.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn, 1400 
    L Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
    
        Date of amendment request: May 17, 1996, as supplemented March 17, 
    1997.
        Description of amendment request: The proposed amendment would 
    modify Technical Specification (TS) Section 3/4.4.5, Steam Generators, 
    3/4.4.6, Reactor Coolant System Leakage, and associated Bases to allow 
    the installation of tube sleeves as an alternative to plugging to 
    repair defective steam generator tubes. The proposed change would also 
    specify the Westinghouse topical reports to be used for sleeve design 
    and inspection, and identify the inspection sample size for repaired 
    tubes. This application was previously published in the Federal 
    Register on May 29, 1996, (61 FR 26938).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Listing the specific Westinghouse topical reports in the 
    TS binds the South Texas Project (STP) to the sleeve design and 
    inspection techniques identified in that revision of the topical 
    report. Any changes to sleeve design or inspection technique would 
    require a separate TS amendment.
        New TS Table 4.4-3, Steam Generator Repaired Tube Inspection, 
    identifies the inspection sample size for steam generator tubes that 
    have already been repaired. This table simply identifies inspection 
    criteria and associated actions for repaired tubes and does not 
    increase the probability or consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. Implementation of laser welded sleeving maintains overall 
    tube bundle structural and leakage integrity conditions. Providing 
    specific Westinghouse topical report references in the TS only 
    serves to identify which sleeve design and inspection techniques are 
    being employed at STP. Likewise, the addition of Table 4.4-3 
    clarifies the expected inspection samples for previously repaired 
    tubes. The addition of Table 4.3-3 provides assurance that 
    previously repaired tubes will be inspected at regular intervals and 
    appropriate action taken if the tube is found defective. Neither of 
    these additions to the TS will create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety. Both of these changes are being added to 
    clarify the STP steam generator tube inspection program and provide 
    more specific detail regarding steam generator tube inspection 
    samples and inspection techniques. By requiring inspection of 
    previously repaired tubes, the margin of safety is increased rather 
    than decreased.
    
    [[Page 17236]]
    
        Based on this review, it appears that the three standards of 10 
    CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
    
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869.
        NRC Project Director: William D. Beckner.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
    
        Date of amendment request: January 28, 1997.
        Description of amendment request: The proposed amendment would 
    relocate the details of Technical Specification (TS) Section 6.2.3 on 
    the Independent Safety Engineering Group (ISEG) from the Administration 
    Controls section of the TSs and place these details in the Updated 
    Final Safety Analysis Report (UFSAR) for South Texas Project, Units 1 
    and 2. This relocation is administrative only, and would not render any 
    changes to the existing plant philosophy toward the ISEG or any safety 
    analysis. Section 6.2.3 would be deleted from the TSs and removed from 
    the table of contents for Administrative Controls. Currently UFSAR 
    Section 13.4.2.2 describes the ISEG, but not in the detail as the 
    current TSs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes move details from the Technical 
    Specifications [TSs] to the Updated Final Safety Analysis Report 
    (UFSAR). The changes do not result in any hardware or operating 
    procedure changes. The details being removed from the Technical 
    Specifications [TSs] are not assumed to be an initiator of any 
    analyzed event. The UFSAR, which will contain the removed Technical 
    Specification [TS] details, will be maintained using the provisions 
    of 10 CFR 50.59 and is subject to the change control process in the 
    Administrative Controls Section of the Technical Specifications 
    [TSs]. [In addition] any changes to the UFSAR will be evaluated per 
    10 CFR 50.59, no increase in the probability or consequences of an 
    accident previously evaluated will be allowed without prior NRC 
    [Nuclear Regulatory Commission] approval. Therefore, the changes do 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes move details from the technical 
    Specifications [TSs] to the Updated Final Safety Analysis Report 
    (UFSAR). The changes will not alter the plant configuration (no new 
    or different type of equipment will be installed) or make changes in 
    methods governing plant operation. The changes will not impose 
    different requirements, and adequate control of information will be 
    maintained. The changes will not alter assumptions made in the 
    safety analysis and licensing basis. Therefore, the changes will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes move detail from the Technical 
    Specifications [TSs] to the Updated Final Safety Analysis Report 
    (UFSAR). The changes do not reduce the margin of safety since the 
    relocation of details [is an administrative action and] has no 
    impact on any safety analysis assumptions. In addition, the detail 
    transposed from the Technical Specifications [TSs] to the UFSAR are 
    the same as the existing Technical Specification [TS] [6.2.3]. [In 
    addition] any future changes to the FSAR will be evaluated per the 
    requirements of 10 CFR 50.59, no reduction in a margin of safety 
    will be allowed without prior NRC approval. [Therefore, the licensee 
    concluded that the changes will not involve a significant reduction 
    in a margin of safety.]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges, Learning Center, 911 Boling Highway, Wharton, TX 77488.
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869.
        NRC Project Director: William D. Beckner.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit No. 1, New London, Connecticut
    
        Date of amendment request: February 7, 1997.
        Description of amendment request: The proposed Technical 
    Specification changes would clarify and/or modify instrument 
    calibration, functional, and response time requirements for resistance 
    temperature detector and thermocouple testing. Also, certain 
    definitions would be clarified and/or modified using applicable wording 
    from NRC's NUREG-1433, ``Standard Technical Specifications,'' Revision 
    1, and industry recommendations. Additionally, the change would 
    relocate the reactor protection system logic response time value 
    utilizing the guidance provided by NRC's Generic Letter 93-08, 
    ``Relocation of Technical Specification Tables of Instrument Response 
    Time Limits,'' with the exception of relocating the value to the 
    Technical Specifications Bases Section instead of the Updated Final 
    Safety Analysis Report. The proposed amendment is intended to clarify 
    instrumentation surveillance requirements, thereby helping to ensure 
    proper testing of safety-related components.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Pursuant to 10 CFR 50.92, NNECO [Northeast Nuclear Energy 
    Company] has reviewed the proposed changes and concludes that the 
    changes do not involve a significant hazards consideration (SHC) 
    since the proposed changes satisf[y] the criteria in 10 CFR 
    50.92(c). That is, the proposed changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed amendment continues to ensure the surveillance 
    requirements satisfy the licensing basis. The current TS [technical 
    specifications] definition for Instrument Functional Test requires 
    injection of a simulated signal into the primary sensor to verify 
    proper response. Current TS exempt the sensors of specific 
    instrument channels where it is not practical to include them within 
    the functional test boundaries. Some examples of these exemptions 
    include neutron monitoring system, turbine control valve fast 
    closure, and standby gas treatment initiation radiation monitors. In 
    these cases, TS permit the performance of the functional test by 
    injection of a simulated electrical signal into the measurement 
    channel. The proposed definition, which is consistent with the STS 
    [standard technical specifications]
    
    [[Page 17237]]
    
    definition, for CHANNEL FUNCTIONAL TEST requires injection of the 
    simulated signal ``as close to the sensor as practicable.'' 
    Therefore, the proposed definition is consistent with the current TS 
    definition and its exemptions. The primary sensor is the transmitter 
    or switch or radiation monitor. The definition does not include 
    sensing elements such as radiation detectors, flow elements, 
    acceleration relays or reference legs.
        This change will allow the channel functional test to be 
    performed by means of any series of sequential, overlapping, or 
    total channel steps and aligns this methodology with industry 
    practice. This change does not affect accident precursors and thus 
    does not involve a significant increase in the probability of an 
    accident previously evaluated. The proposed change will allow a 
    simulated or actual signal to be used to perform an Instrument or 
    Channel Functional Test. This change does not impose a requirement 
    to create an actual signal, nor does it eliminate any restriction on 
    producing an actual signal. While creating an ``actual'' signal 
    could increase the probability of an event, existing procedures (and 
    the 10 CFR 50.59 control of revisions to them) dictate the 
    acceptability of generating this signal. The proposed change does 
    not affect the procedures governing plant operations or the 
    acceptability of creating these signals; it simply would allow such 
    a signal to be utilized in evaluating the acceptance criteria for 
    the Instrument or Channel Functional Test requirements. Therefore, 
    the change does not involve a significant increase in the 
    probability of an accident previously evaluated. Because the method 
    of initiation will not affect the acceptance criteria of the 
    Instrument or Channel Functional Test, the change does not involve a 
    significant increase in the consequences of an accident previously 
    evaluated.
        Minor word differences from STS are required to provide 
    consistency with current TS wording and support the current 
    licensing basis. These minor word differences including Industry/
    TSTF [Technical Specification Task Force] Standard Technical 
    Specification Change Traveler (TSTF-64) do not alter the meaning of 
    instrument testing in the STS or change the current licensing basis.
        Moving the RPS [Reactor Protection System] Logic Response Time 
    LCO [Limiting Condition of Operation] description to the TS 
    definition section is an administrative change and does not alter 
    the original intent or licensing basis.
        Relocation of the RPS Logic Response Time value from the TS to 
    the Bases section involves the use of an alternate regulatory 
    process for controlling the instrument response time limit. The 
    change does not introduce any new modes of plant operation, make any 
    physical changes, alter any operational setpoints, or change the 
    surveillance requirements. Any change in the RPS logic response time 
    value would be evaluated pursuant to the requirements of 10 CFR 
    50.59.
        The surveillance section editorial change does not alter the 
    meaning of surveillance applicability. Providing RPS Logic Response 
    Time surveillance frequency and applicable trip functions ensures 
    proper testing of RPS components and is consistent with industry 
    practice. An evaluation completed by GE [General Electric] verified 
    the applicable RPS trip functions that require a specific logic 
    response time using the current accident analysis as the basis. For 
    trip functions where no explicit credit is taken in the safety 
    analysis, the measurement of logic response time is not important, 
    and therefore, not warranted. In addition, we have concluded, that 
    instrumentation response time requirements (specified limits) other 
    than RPS logic are not important to test, especially considering the 
    long delays already accounted for in the accident analyses 
    associated with the start of emergency power sources, ECCS 
    [Emergency Core Cooling System] components, and containment 
    isolations, and that the non-RPS logic response times, including 
    response times of other instrumentation such as radiation monitors, 
    are not part of the Millstone Unit No. 1 licensing basis. The 
    sensors associated with all TS instrumentation are functionally 
    tested and calibrated to ensure proper operation.
        No physical change is being made to instrument channels, or to 
    any systems or component that interfaces with the instrumentation 
    channels, therefore there is no change in the probability or 
    consequences of any accident analyzed in the UFSAR [Updated Final 
    Safety Analysis Report].
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed change does not result in any design or physical 
    configuration changes to the instrumentation channels. Operation 
    incorporating the proposed change will not impair the 
    instrumentation channels from performing as provided in the design 
    basis.
        Changing the TS to be consistent with current industry practice 
    adopted in STS will help to prevent unnecessary removal and 
    potential damage of the temperature detectors (for sensor 
    calibration). Clarification of RPS Logic Response Time testing 
    requirements consistent with the current licensing basis will ensure 
    proper testing of safety-related components.
        Wording changes to Instrument Calibration and Functional Test 
    definitions do not involve a physical modification to the plant. The 
    injection of an actual or simulated signal as close to the sensor as 
    practical minimizes the likelihood of any transients.
        Minor word differences from STS are required to provide 
    consistency with current TS wording and support the current 
    licensing basis. These minor word differences, including Industry/
    TSTF Standard Technical Specification Change Traveler (TSTF-64), do 
    not alter the meaning of instrument testing in the STS or change the 
    current licensing basis.
        Moving the RPS Logic Response Time LCO description to the TS 
    definition section is an administrative change and does not alter 
    the current licensing basis.
        Relocation of the RPS Logic Response Time value involves the use 
    of an alternate process for controlling the instrument response time 
    limits. Therefore, the above change does not introduce any accident 
    initiators as it does not involve any new modes of plant operation, 
    make any physical changes, alter any operational setpoints, or 
    change the surveillance requirements.
        The surveillance section editorial change does not alter the 
    meaning of surveillance applicability. Providing RPS Logic Response 
    Time surveillance frequency and applicable trip functions ensures 
    proper testing of RPS components and is consistent with industry 
    practice.
        Since the proposed changes in the Technical Specifications do 
    not adversely impact the reliability of the RPS and other automatic 
    actuations, no new or different kind of accident is created.
        3. Involve a significant reduction in a margin of safety.
        Because the proposed change does not involve the addition or 
    modification of plant equipment, is consistent with the existing 
    Technical Specifications, current industry practices as outlined in 
    NUREG 1433, ``Standard Technical Specifications GE Plants, BWR/4,'' 
    Revision 1, and with the current design and licensing basis of the 
    Protective Instrumentation systems including the accident analysis, 
    no action will occur that will involve a significant reduction in a 
    margin of safety.
        The proposed change to allow the use of an actual signal in 
    addition to the existing requirement, which limits use to a 
    simulated signal, will not affect functional test acceptance 
    criteria. Therefore, the proposed change does not adversely affect 
    the reliability of the RPS or other automatic actuation and does not 
    involve a significant reduction in a margin of safety.
        Relocation of the RPS Logic Response Time value from the TS to 
    the Bases section involves the use of an alternate regulatory 
    process for controlling the instrument response time limit. Any 
    change in the RPS logic response time value would be evaluated 
    pursuant to the requirements of 10 CFR 50.59.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis, and based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
    
    [[Page 17238]]
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of amendment request: November 25, 1996, as supplemented 
    December 12, 1996.
        Description of amendment request: The proposed amendment would make 
    changes to Section 2.1.A for the Safety Limit Minimum Critical Power 
    Ratio (SLMCPR) and to Section 3.11.C for the Operating Limit Minimum 
    Critical Power Ratio (OLMCPR). The proposed change to Section 2.1.A 
    revises the SLMCPR value from 1.07 to 1.08 for two recirculation pump 
    operation and from 1.08 to 1.09 for single loop operation. The proposed 
    change to Section 3.11.C deletes the sentence that specifies the OLMCPR 
    limit penalty for single recirculation loop operation and adds a 
    statement that references the Core Operating Limits Report (COLR) as 
    the source for this information.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The basis of the MCPR [minimum critical power ratio] Safety 
    Limit calculation is to ensure that greater than 99.9% of all fuel 
    rods in the core avoid transition boiling if the limit is not 
    violated. The new SLMCPRs preserve the existing margin to transition 
    boiling and fuel damage in the event of a postulated accident. The 
    probability of fuel damage is not increased. The derivation of the 
    revised SLMCPRs for Monticello for incorporation into the Technical 
    Specification, and its [their] use to determine cycle-specific 
    thermal limits, have been performed using NRC-approved methods as 
    identified in Technical Specification 6.7.A.7.b. NSP [Northern 
    States Power] methodology established OLMCPR such that integrity of 
    the SLMCPR is maintained for the bounding analyzed transients. 
    Additionally, GENE [General Electric Nuclear Energy] interim 
    implementing procedures, which incorporate cycle-specific 
    parameters, have been used. Based on the use of these calculations, 
    the calculation of the revised SLMCPRs maintains the integrity of 
    the safety limits and therefore cannot increase the probability or 
    severity of an accident. The single loop OLMCPR evaluation was 
    performed using NSP methodology approved by the NRC. Relocating the 
    OLMCPR value to the COLR establishes appropriate control on a core 
    operating limit which may vary from cycle to cycle because it is 
    cycle dependent. Since OLMCPR is developed using procedures approved 
    in the Technical Specifications, placing the OLMCPR in the COLR 
    cannot result in a change not controlled by the Technical 
    Specifications. The change does not affect failure modes of 
    equipment, therefore, this amendment will not cause a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The MCPR Safety Limit is a Technical Specification numerical 
    value, designed to ensure that fuel damage from transition boiling 
    does not occur as a result of the limiting postulated accident. It 
    cannot create the possibility of any new type of accident. The new 
    SLMCPRs have been calculated using NRC-approved methods and the 
    OLMCPR values are more conservative. Additionally, interim 
    procedures, which incorporate cycle-specific parameters, have been 
    used. Therefore, the proposed Technical Specification change does 
    not create the possibility of a new or different kind of accident, 
    from any accident previously evaluated.
        3. The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The MCPR Safety Limit is a Technical Specification numerical 
    value, designed to ensure that fuel damage from transition boiling 
    does not occur as a result of the limiting postulated accident. 
    Increasing the SLMCPR and OLMCPR values results in an increase in 
    the margin of safety to fuel failure, and does not affect other 
    plant systems. Therefore, the proposed Technical Specification 
    change does not involve a significant reduction in the margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: November 20, 1996, as supplemented by 
    letter dated February 20, 1997.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to allow the Vice President to 
    designate the Safety Audit and Review Committee (SARC) Chairperson, to 
    change the work hours limitation in accordance with guidance in GL 82-
    12, ``Nuclear Power Plant Staff Working Hours;'' to change radioactive 
    shipments record retention requirements to comply with recent 10 CFR 
    Part 20 changes; to revise position titles to reflect organizational 
    changes; and other editorial changes. The February 20, 1997, 
    supplemental letter differs from the November 20, 1996, application 
    which was noticed in the Federal Register on January 2, 1997 (62 FR 
    131), in that the previous application did not propose changes to TS 
    5.3, 5.5, 5.6, 5.7, and 5.11 reflecting recent organizational changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The changes requested are administrative in nature. Paragraph 
    3.D was placed in the License by Amendment No. 155 to authorize 
    Omaha Public Power District (OPPD) to increase the storage capacity 
    of the FCS spent fuel pool. Amendment No. 155 stated that the TS as 
    issued would be effective when the last new rack was installed. 
    Since the last new rack was installed on August 8, 1994, Paragraph 
    3.D is no longer necessary and should be deleted from the License.
        Table of Contents, Section 6.0, ``Interim Special Technical 
    Specifications,'' Subsections 6.1 through 6.4 are proposed for 
    deletion because all of the Specifications referred to have been 
    deleted by previous Amendments.
        The revision proposed for TS 2.15 (Item 2C of Table 2-3 & Item 
    1C of Table 2-4) will insert the correct terminology (Pressurizer 
    Low/Low Pressure) into the Functional Unit description.
        The revision proposed for TS 5.2 will delete the specific 
    working hours as stated and relocate these requirements to the 
    Updated Safety Analysis Report (USAR). Overtime will remain 
    controlled by plant administrative procedures with the USAR 
    generally following the guidance of the NRC's Policy Statement on 
    working hours contained in Generic Letter 82-12, ``Nuclear Power 
    Plant Staff Working Hours.'' Specifying personnel working hours in 
    TS does not meet any of the four criteria contained in 10 CFR 50.36 
    for inclusion in the TS. Revisions to plant procedures containing 
    these requirements are required to be evaluated in accordance with 
    10 CFR 50.59. The proposed relocation is similar to recent 
    Amendments issued to the Davis-Besse Nuclear Power Station and the 
    San Onofre Nuclear Generating Station.
        The revision proposed for TS 5.5.2.2 will replace the specific 
    title of the Chairperson of the Safety Audit and Review Committee
    
    [[Page 17239]]
    
    and replace it with ``Member as appointed by the Vice President.'' 
    This will allow the flexibility to change chairmanship of the 
    committee amongst the members.
        The revisions proposed to TS 5.3, 5.5, 5.6, 5.7, and 5.11 revise 
    position titles and reporting responsibilities to reflect 
    organizational changes. Qualifications for individuals in these 
    positions meet or exceed the previous requirements.
        The revision to TS 5.10 concerning retention of records of 
    radioactive shipments will update the TS to current 10 CFR 20 
    requirements. Plant procedures already comply with current 10 CFR 20 
    record retention requirements. The addition of the Section 5.0 title 
    corrects a minor format discrepancy.
        These proposed revisions are administrative in nature. The 
    proposed revisions have no effect on any initial assumptions or 
    operating restrictions assumed in any accident, nor do these changes 
    have any effect on equipment required to mitigate the consequences 
    of an accident. Therefore the proposed revisions do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed revisions correct minor errors, remove outdated 
    information, are consistent with changes in organizational 
    structure, 10 CFR Part 20, or the criteria contained in 10 CFR 
    50.36. These changes will not result in any physical alterations to 
    the plant configuration, changes to setpoint values, or changes to 
    the application of setpoints or limits. No new operating modes are 
    proposed as a result of these changes. Therefore the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The revisions listed above correct minor errors, remove outdated 
    information, or are consistent with changes in organizational 
    structure, 10 CFR Part 20, or the criteria contained in 10 CFR 
    50.36. These changes will not result in any physical alterations to 
    the plant configuration, changes to setpoint values, or changes to 
    the application of setpoint or limits. Therefore the proposed 
    changes do not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of amendment request: February 26, 1997.
        Description of amendment request: The proposed amendment would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant, Unit Nos. 1 and 2 to revise TS 3/4.4.5 and 3.4.6.2, 
    including associated Bases 3/4.4.5 and 3/4.4.6.2, to allow the 
    implementation of steam generator (SG) tube voltage based repair 
    criteria for outside diameter stress corrosion cracking (ODSCC) 
    indications at tube-to-tube support plate (TSP) intersections. The 
    allowed primary-to-secondary operational leakage from any one SG would 
    be reduced from 500 gpd to 150 gpd.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
    
    Structural Integrity Considerations
    
        The structural criteria ensure that all indications subjected to 
    voltage-based repair limits will be able to withstand pressure 
    loading consistent with the criteria of NRC Regulatory Guide (RG) 
    1.121.
        Tube burst criteria are inherently satisfied during normal 
    operating conditions because of the proximity of the tube support 
    plate (TSP). It is conservatively assumed that the entire crevice 
    region is uncovered during the secondary side blowdown of a main 
    steam line break (MSLB). Therefore, during a postulated MSLB 
    accident, tube burst capability must exceed the RG 1.121 criterion 
    requiring a margin of 1.43 times the steam line break pressure 
    differential on tube burst.
        Based on the latest industry database, the RG 1.121 criterion is 
    satisfied by bobbin coil indications of outside diameter stress 
    corrosion cracking (ODSCC) with signal amplitudes less than 8.7 
    volts. The latest NRC-approved database will be used for repair and 
    analysis applications.
        Industry testing of model boiler and operating plant tube 
    specimens for free-span tubing (no tube support plate (TSP) 
    restraint) at room temperature conditions show typical burst 
    pressures in excess of 5,000 psi for ODSCC indications with voltage 
    measurements at or below 8.7 volts. This tube burst capability 
    exceeds the RG 1.121 criterion.
        The lower voltage repair limit is conservatively defined to be 
    2.0 volts in accordance with NRC Generic Letter (GL) 95-05, 
    ``Voltage-Based Repair Criteria for Westinghouse Steam Generator 
    Tubes Affected by Outside Diameter Stress Corrosion Cracking,'' 
    August 3, 1995. This 2.0 volt repair limit is very conservative 
    because it contains a large safety margin, based on a structural 
    limit of 8.7 volts. A maximum allowable upper repair limit (URL) is 
    also established using the guidance of GL 95-05. The URL is 
    calculated before each inspection by subtracting the NDE uncertainty 
    and growth rate allowances from the current structural limit. The 
    URL for near term inspections at DCPP Units 1 and 2 is expected to 
    be about 5.0 volts. Bobbin indications greater than 2.0 volts and 
    less than or equal to 5.0 volts that are confirmed by RPC will be 
    repaired. Bobbin indications greater than 5.0 volts will be 
    repaired.
        Following each inspection, burst probability analyses are 
    performed for the end of cycle (EOC) distribution. In accordance 
    with GL 95-05, the projected MSLB burst probability must be less 
    than the threshold value of 1 x 10 x 2. Based on the relatively 
    small number and voltages of ODSCC indications identified to date at 
    DCPP Units 1 and 2, it is expected that the near term EOC 
    conditional burst probability for a faulted SG will be much less 
    than this threshold value, providing further assurance of acceptable 
    structural integrity.
    
    Leakage Considerations
    
        PG&E will implement reduced operational leakage limits as 
    recommended in GL 95-05. PG&E will revise the TS to implement a 
    maximum leakage rate of 150 gpd for any one SG to help preclude the 
    potential for excessive leakage during power operation in Modes 1 
    and 2. The TS has also been changed to specify that the 150 gpd leak 
    limit is not necessarily a limiting condition for operation in Modes 
    3 and 4. The 150 gpd leak rate per steam generator has been 
    established for normal operation. This leakage rate provides added 
    assurance against tube rupture at normal and faulted conditions. In 
    Modes 3 and 4, there is less differential pressure across the tube 
    and the potential source term from a tube failure is much less than 
    in Modes 1 and 2. The operational leak rate monitoring program is a 
    defense-in-depth measure that provides a means for identifying leaks 
    during power operation to allow for repair before such leaks can 
    result in tube failure. The leakage criteria ensure that for 
    indications subjected to voltage-based repair criteria, induced 
    leakage under worst-case MSLB conditions will not result in offsite 
    and control room dose releases that exceed the applicable guideline 
    values of 10 CFR 100 and GDC 19.
        Relative to the expected leakage during accident condition 
    loadings, a postulated MSLB outside of containment, but upstream of 
    the main steam isolation valve (MSIV), represents the most limiting 
    radiological condition for implementation of voltage-based repair 
    criteria. The steam generator tubes are subjected to an increase in 
    differential pressure following a MSLB, resulting in a postulated 
    increase in leakage
    
    [[Page 17240]]
    
    and associated offsite doses. Leakage following a MSLB bypasses 
    containment.
        PG&E will calculate the primary-to-secondary leakage for 
    degradation subjected to the voltage repair criteria under worst-
    case postulated MSLB conditions. The leak rate will be compared to 
    the maximum allowable leak rate limit of 12.8 gpm to ensure that a 
    postulated MSLB occurring at EOC would not result in radiological 
    consequences that are in excess of the applicable offsite and 
    control room dose guidelines of 10 CFR 100 and GDC 19. Based on the 
    relatively small number of ODSCC indications identified to date at 
    DCPP Units 1 and 2, it is expected that the near term EOC predicted 
    leak rates for a faulted SG will be much less than the maximum 
    allowable leak rate limit.
        Therefore, based on the structural integrity and leakage 
    considerations discussed above, the proposed changes do not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Implementation of the proposed voltage-based repair criteria for 
    ODSCC at TSP intersections does not introduce any significant change 
    to the plant design basis. Use of the criteria does not create a 
    mechanism which could result in an accident in the free span because 
    the repair criteria do not apply to tubes containing ODSCC located 
    outside the thickness of the TSPs. Based on the burst probability 
    acceptance limit of 1 x 10-2, it is expected that for all plant 
    conditions, neither a single nor multiple tube rupture event would 
    likely occur in a steam generator where voltage-based repair 
    criteria have been applied.
        Steam generator tube integrity is continually maintained through 
    inservice inspection and primary-to-secondary leakage monitoring. 
    Any tubes with ODSCC degradation in excess of the URL are repaired.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The use of the bobbin probe to disposition ODSCC degraded tubes 
    within TSP intersections by voltage-based repair criteria is 
    demonstrated to maintain SG tube integrity in accordance with the 
    requirements of RG 1.121. RG 1.121 describes a method acceptable to 
    the NRC Staff for meeting GDCs 14, 15, 31, and 32 by reducing the 
    probability or the consequences of SG tube rupture. This is 
    accomplished by determining the limiting conditions of degradation 
    of SG tubing, as established by inservice inspection, for which 
    tubes with unacceptable degradation are removed from service. Upon 
    implementation of the voltage-based repair criteria, even under the 
    worst case conditions, the occurrence of ODSCC at TSP intersections 
    is not expected to lead to a SG tube rupture during normal or 
    faulted plant conditions, nor is it expected to lead to unacceptable 
    primary-to-secondary leakage.
        In addressing the combined effects of a loss of coolant accident 
    (LOCA) and safe shutdown earthquake (SSE) on the SGs, as required by 
    GDC 2, it has been determined that tube collapse may occur based on 
    analysis for a large break LOCA plus SSE. The analysis identifies a 
    maximum of 7.5 percent of tubes per SG located adjacent to wedge 
    regions that are subject to potential collapse during combined LOCA 
    and SSE. Tubes located in the wedge region exclusion zone will be 
    excluded from application of voltage-based repair criteria. Thus, 
    existing tube integrity requirements apply to these tubes and the 
    margin of safety is not reduced.
        Implementation practices using voltage-based repair criteria 
    bounds RG 1.83 considerations. Specifically, GL 95-05 requires the 
    following: (1) enhanced eddy current inspection guidelines are 
    implemented to provide consistency in voltage normalization; (2) 100 
    percent bobbin coil inspections are performed each cycle for all hot 
    leg TSP intersections and all cold leg TSP intersections down to the 
    lowest cold leg TSP with known ODSCC indications; and (3) rotating 
    pancake coil (RPC) inspection of indications greater than 2 volts 
    are performed to characterize the principal degradation as ODSCC. 
    DCPP's proposed voltage-based repair criteria implementation 
    practices meet the above requirements, and in some areas exceed them 
    (for example, 100 percent bobbin coil inspections are routinely 
    performed each cycle on every TSP intersection).
        Implementation of voltage-based repair criteria at TSP 
    intersections will decrease the number of tubes which must be 
    repaired. Since the installation of tube plugs to remove ODSCC 
    degraded tubes from service reduces RCS flow margin, voltage-based 
    repair criteria implementation will help preserve the margin of RCS 
    flow.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: William H. Bateman.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: February 27, 1997.
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant, Unit Nos. 1 and 2 by revising Technical Specifications 
    (TS) 3/4.8.1.1, ``A.C. Sources--Operating,'' to clarify that emergency 
    diesel generator (EDG) testing is initiated from standby conditions 
    rather than ``ambient'' conditions. The associated TS Bases will be 
    revised to discuss the temperature range that satisfies EDG standby 
    conditions. This amendment also proposes to revise TS 3/4.3.2, 
    ``Instrumentation--Engineering Safety Features Actuation System 
    Instrumentation.'' This revision clarifies that when one or both of the 
    first level load shed relays, or one or both of the second level 
    undervoltage relays are inoperable, the associated EDG for that bus 
    shall be declared inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes to the technical specifications (TS) do not 
    change the function or operation of any plant equipment or affect 
    the response of that equipment if it is called upon to operate.
        The proposed change to TS 4.8.1.1.2a.2 and the Bases will 
    clarify the term ``ambient conditions'' as used in the emergency 
    diesel generator (EDG) surveillance requirement. EDG testing will 
    still be completed on a frequency commensurate with the current TS.
        The proposed change to TS 3.3.2, Table 3.3-3, will permit time 
    to restore the load shed first level undervoltage relays (FLURs) and 
    second level undervoltage relays (SLURs) to operable status that is 
    consistent with times allowed for outage of other safety-related 
    equipment affecting one train of vital equipment. This proposed 
    change maintains a high degree of equipment availability without 
    requiring unnecessary initiation of a plant shutdown for partial 
    equipment outages.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of
    
    [[Page 17241]]
    
    accident from any accident previously evaluated.
        The proposed change to TS 4.8.1.1.2a.2 and the Bases will 
    clarify the term ``ambient conditions'' as used in the EDG 
    surveillance requirement. EDG testing will still be completed on a 
    frequency commensurate with the current TS, and will be more 
    representative of the conditions under which the EDGs would be 
    required to start in an accident condition.
        The proposed change to TS 3.3.2, Table 3.3-3, will provide time 
    to restore the load shed FLURs and SLURs to operable status that is 
    consistent with times allowed for outage of other safety-related 
    equipment affecting one train of vital equipment. The load shed FLUR 
    and SLUR sets for one 4 kV bus only affect one train of vital 
    equipment. If an accident occurred while the relays were inoperable, 
    the redundant trains (two remaining EDGs and vital buses) would 
    complete the safety function. The proposed allowed outage time (AOT) 
    for the load shed FLURs and SLURs is bounded by the time allowed for 
    an EDG supporting the vital 4 kV bus and is consistent with AOTs for 
    other safety-related components.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change to TS 4.8.1.1.2a.2 and its Bases, clarifies 
    the term ``ambient conditions'' as used in the EDG surveillance 
    requirement. EDG testing will still be completed on a frequency 
    commensurate with the current TS. Use of temperatures in the standby 
    range result in no significant variation in EDG start times as 
    indicated by the diesel vendor and by PG&E test results. Standby 
    conditions are representative of actual starting conditions that 
    would be in effect if the EDGs started in an accident.
        The proposed change to TS 3.3.2, Table 3.3-3, will provide time 
    to restore the load shed FLURs and SLURs to operable status that is 
    consistent with times allowed for outage of other safety-related 
    equipment affecting one train of vital equipment. If an accident 
    occurred while the relays were inoperable, the redundant trains (two 
    remaining EDGs and vital buses) would complete the safety function. 
    The proposed change eliminates an unneccessary plant shutdown and 
    associated risk due to shutdown transient. It prevents a transient 
    that could require the EDGs at a time when less than all three EDGs 
    would be operable.
        Therefore, neither of the proposed changes involves a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120.
        NRC Project Director: William H. Bateman.
    
    Portland General Electric Company, et al., Docket No. 50-344, 
    Trojan Nuclear Plant, Columbia County, Oregon
    
        Date of amendment request: January 28, 1997.
        Description of amendment request: The proposed amendment by 
    Portland General Electric (PGE or the licensee) clarifies the 
    administrative controls that are used for the revision and maintenance 
    of the Certified Fuel Handler Training Program. The change allows the 
    licensee to make changes to the certified fuel handlers program without 
    prior NRC staff approval. The text of the proposed change is taken from 
    the improved standard technical specifications, NUREG-1431, ``Standard 
    Technical Specifications, Westinghouse Plants.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        In accordance with the requirements of 10 CFR 50.92, ``Issuance 
    of amendment,'' this license amendment request is judged to involve 
    no significant hazards consideration based upon the following:
        1. The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change is a clarification of the method of control 
    that will be used for the Certified Fuel Handler Training Program, 
    and as such, is administrative in nature and has no impact on the 
    probability or consequences of accidents previously evaluated. The 
    physical structures, systems, and components of the facility and the 
    operating procedures for their use are unaffected by this proposed 
    clarification. The proposed administrative controls provide adequate 
    confidence that personnel that perform the certified fuel handler 
    functions will have been adequately trained for the changing 
    conditions of the facility. Since the training program will prepare 
    the operations personnel for fuel handling operations, including 
    responses to abnormal events/accidents, there will be no increase in 
    the probability of occurrence or in the consequences of an accident 
    previously evaluated.
        2. The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        This change ensures the qualifications of the operations 
    personnel are commensurate with the tasks to be performed and the 
    conditions to which they may be required to respond. This change 
    does not affect plant equipment or the procedures for operating 
    plant equipment and, therefore, does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in a margin of safety.
        This change ensures the qualification of the operations 
    personnel are commensurate with the tasks to be performed and the 
    conditions to which they may be required to respond. The assumptions 
    for a fuel handling accident in the Fuel Building are not affected 
    by the proposed change. The proposed amendment does not, therefore, 
    involve a reduction in a margin of safety.
    
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
        Attorney for the Licensees: Leonard A. Girard, Esq., Portland 
    General Electric Company, 121 S.W. Salmon Street, Portland, Oregon 
    97204.
        NRR Project Director: Seymour H. Weiss.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: September 11, 1996.
        Description of amendment request: The proposed amendment would 
    permit operation with increased safety relief valve (SRV) and safety 
    valve (SV) setpoint tolerance and permit operation up to 100% of rated 
    power with a single inoperable SRV.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed changes will permit operation with increased SRV 
    and SV setpoint tolerance and permit operation up to 100% of rated 
    power with a single inoperable SRV.
    
    [[Page 17242]]
    
        The valves are not related to the control rod system. The valves 
    are not involved in the initiation of a Control Rod Drop Accident. 
    The valves are part of the Reactor Vessel (RV) pressure boundary and 
    their failure could initiate a LOCA [loss-of-coolant accident]. 
    However, the proposed changes do not constitute a change in the 
    design of the valves from a pressure boundary perspective. The 
    proposed changes do not affect the probability of a LOCA initiated 
    by valve failure. The valves are not a component, system, or 
    structure involved in refueling operations. The valves and their as-
    found setpoint tolerance are not involved in the initiation of a 
    Refueling Accident.
        The design basis Main Steam Line Break is a complete severance 
    of one main steam line outside the secondary containment. The SRVs 
    and SVs are located inside primary containment and cannot cause a 
    main steam line rupture outside secondary containment. The valves 
    are not involved in the initiation of a design basis Main Steam Line 
    Break. The probability or consequences of these accidents are not 
    affected.
        Attachment C [see application dated September 11, 1996] includes 
    an analysis to demonstrate that margin exists to SV challenges 
    during an Abnormal Operational Transient (AOT). For this purpose a 
    Generator Load Rejection without Bypass (GLRWOBP) was identified as 
    the limiting AOT. The results confirm that SV challenges would not 
    occur with an inoperable SRV at rated power.
        The current Technical Specification limit of 95% rated power or 
    less with an inoperable SRV is therefore not required to prevent SV 
    challenges during an AOT.
        As discussed in Attachment C [see application], the impact of 
    the proposed as-found SRV setpoint tolerance increase on SRV piping/
    supports and discharge loads to the Torus was evaluated. A 
    mechanical loads analysis confirmed the integrity of these 
    components, systems, and structures during SRV discharge with the 
    proposed changes.
        Attachment C [see application] provides an evaluation of the 
    impact of the proposed changes on the consequences of the Loss of 
    Coolant Accident and the Main Steam Line Break. The limiting LOCA 
    event is a break in the recirculation loop, with a break area of 0.6 
    ft\2\, at the pump discharge location, with a loss of one train of 
    DC power as the single failure. For breaks in the recirculation line 
    larger than 0.4 ft\2\, the SRVs would not be challenged. Therefore, 
    in assessing the impact of the proposed changes on 10CFR50.46 
    acceptance criteria, only recirculation line breaks less than 0.4 
    ft\2\ were reevaluated. Results show that the 0.6 ft\2\ 
    recirculation line break remains the limiting LOCA event and it is 
    not affected. The consequences of the limiting design basis LOCA are 
    not increased by the proposed changes. The design basis accident for 
    containment performance is a double-ended break in the recirculation 
    pump suction. For this size break, the SRVs are not challenged. 
    Therefore, the proposed changes do not have any effect on the design 
    basis accident for containment performance. The design basis 
    accident for radioactive material releases and radiological effects 
    is a complete severance of one main steam line outside the secondary 
    containment. For steam line breaks outside the containment, MSIVs 
    [main steam isolation valves] close and terminate radiological 
    releases outside the containment, SRVs are not challenged until 
    after MSIV closure and isolation. Therefore, the proposed changes do 
    not increase the radiological consequences of the design basis Main 
    Steam Line Break.
        The SRVs and SVs are designed to mitigate the consequences of 
    malfunctions of equipment which result in a Nuclear System pressure 
    increase. These abnormal operational transients are defined and 
    analyzed in Section 14.5.1 of the VY [Vermont Yankee] FSAR [final 
    safety analysis report]. The impact of the proposed changes on these 
    abnormal operational transients was evaluated. Results are 
    documented in Attachment C [see application] and show that 
    applicable acceptance criteria are met provided operating MCPR 
    [minimum critical power ratio] limits as specified in the COLR [core 
    operating limit report] are adjusted to reflect the effects of the 
    proposed changes. A hot channel analysis of the limiting delta CPR 
    overpressure transient confirmed that a 0.02 increase in the 
    operating MCPR limits bounds the combined effects of implementing 
    the proposed changes in the current cycle. The operating MCPR limits 
    in COLR have already been increased for the current cycle. 
    Appropriate operating MCPR limits for future cycles will be 
    determined from cycle-specific safety analyses performed with the 
    approved changes.
        Current practice regarding SRV setpoints is to assure plus or 
    minus 1% tolerance is met as required by the ASME [American Society 
    of Mechanical Engineers] Boiler & Pressure Vessel Code referenced in 
    Technical Specification Surveillance Requirement 4.6.E.2. As-left 
    setpoints always meet the plus or minus 1% tolerance. The safety 
    analysis in Attachment C [see application] demonstrates that as-
    found setpoints within plus or minus 3% are acceptable. However, 
    valves re-installed after testing will continue, as previously, to 
    meet plus or minus 1% tolerance as required by the ASME Boiler & 
    Pressure Vessel Code. Thus, the probability of SRV actuation (and 
    the associated risk of failure to reseat properly) is not increased 
    by the proposed change.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from an accident previously 
    evaluated.
        The proposed changes will permit operation with increased Safety 
    Relief Valve (SRV) and Safety Valve (SV) setpoint tolerance and 
    permit operation up to 100% of rated power with a single inoperable 
    SRV. The proposed changes:
        (1) do not constitute a change in the design of the valves;
        (2) will not cause the valve or associated systems and 
    structures to be operated beyond their original design envelopes; 
    and,
        (3) do not involve new plant equipment.
        Therefore, this amendment does not create the possibility of a 
    new or different kind of accident.
        3. The proposed amendment will not involve a significant 
    reduction in a margin of safety.
        Technical Specification Basis 3.6 and 4.6D identifies the 
    minimum critical power ratio (MCPR) safety limit. Operational 
    restraints on MCPR are placed in the COLR to assure no violation of 
    the MCPR safety limit during AOTs. The impact of the proposed 
    changes on MCPR limits was determined by performing a hot channel 
    analysis for the overpressure transient which yields the largest 
    transient drop in CPR [critical power ratio] (delta CPR). Results 
    are documented in Attachment C [see application], and show that a 
    0.02 increase in the operating MCPR limits bounds the combined 
    effects of the proposed changes and assures the MCPR safety limit is 
    not violated during AOTs. The margin of safety defined by the MCPR 
    safety limit is not reduced.
        Technical Specification Basis 3.6 and 4.6D also identifies the 
    ASME Boiler and Pressure Vessel Code Section III-A limit which 
    permits pressure transients up to 10% over design pressure (110% x 
    1250 = 1375 psig). This margin of safety is not reduced by the 
    proposed changes. Attachment C [see application] documents new 
    overpressure transient analysis with results that demonstrate the 
    ASME overpressure limit of 110% of design is met. This license 
    amendment request does not propose to reduce the margin of safety 
    defined by the ASME Boiler & Pressure Vessel Code limit.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: R. K. Gad, III, Ropes and Gray, One 
    International Place, Boston, MA 02110-2624.
        NRC Project Director: Patrick D. Milano, Acting.
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: February 3, 1997 as supplemented March 
    18, 1997.
        Description of amendment request: The proposed change to Technical 
    Specification 4.15.B.1 is administrative in nature in that it revises 
    the Technical Specifications (TS) to be consistent with the NRC-
    approved inservice inspection program. In addition, three TS pages 
    which were previously approved by NRC, and which were inadvertently 
    omitted in an earlier amendment (amendments 40 and 39 for units 1 and 
    2, respectively), are being reissued.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the
    
    [[Page 17243]]
    
    issue of no significant hazards consideration, which is presented 
    below:
    
        1. Operation of Surry Units 1 and 2 in accordance with the 
    proposed Technical Specifications change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed change is administrative in nature, and station 
    operations are not being affected. The ASME Section XI Code 
    requirements are thoroughly established, reviewed and approved by 
    ASME, the industry and ultimately endorsed by the NRC for inclusion 
    into 10 CFR 50.55a. Updates to the Code reflect advances in 
    technology and consider information obtained from plant operating 
    experience to provide enhanced inspection and examination techniques 
    for pipe welds. Therefore, performing weld examinations for the pipe 
    in our augmented inspection program to the requirements of the 1989 
    edition of the ASME Section XI Code provides a regulatory acceptable 
    and adequate level of assurance that the integrity of the pipe will 
    be maintained. By not referencing a specific Code edition in the 
    Technical Specifications, our examinations for pipe in the augmented 
    inspection program will consistently be performed to the Code of 
    record, consistent with the requirements [of] 10 CFR 50.55a. 
    Consequently, the probability or consequences of an accident 
    previously evaluated are not increased.
        2. The proposed Technical Specifications change does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        As noted above, the proposed change is administrative in nature, 
    and no new accident precursors are being introduced. Since the 
    augmented inspection program will continue to be performed to NRC 
    approved ASME Section XI Code requirements, adequate assurance is 
    provided to ensure the integrity of the pipe. Consequently, the 
    proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed Technical Specifications change does not involve 
    a significant reduction in a margin of safety.
        Performing weld examinations to the Code of record is prudent, 
    consistent with accepted industry and regulatory requirements, and 
    provides adequate assurance that piping integrity will be 
    maintained. The use of a general ASME Section XI Code reference in 
    Technical Specification 4.15.B.1 is consistent with the existing 
    wording in Technical Specifications 4.15.A and C, and ensures that 
    weld examinations are being consistently performed to the currently 
    approved edition of the ASME Section XI Code. This is an 
    administrative change and as such does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. The staff notes that the reissuance of three TS pages is a 
    purely administrative matter which involves no significant hazards 
    consideration and which has been considered previously. Therefore, the 
    NRC staff proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Mark Reinhart, Acting.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Dates of amendment requests: June 4, 1996, as supplemented August 
    5, September 26, October 21, November 13, November 20, and December 2, 
    1996, and January 16, March 5, and March 20, 1997 (TSCR 188 and 189).
        Description of amendment requests: The proposed amendments would 
    revise License Nos. DPR-24 and DPR-27 to add commitments for control 
    room habitability and revise Technical Specification (TS) Sections 
    15.1, ``Definitions,'' 15.2.1, ``Safety Limit, Reactor Core,'' 15.2.3, 
    ``Limiting Safety System Settings and Protective Instrumentation,'' 
    Section 15.3.1, ``Reactor Coolant System,'' 15.3.4, ``Steam and Power 
    Conversion System,'' 15.3.5, ``Instrumentation System, 15.4.1, 
    ``Operational Safety Review,'' 15.5.3, ``Design Features--Reactor,'' 
    and 15.6.9, ``Plant Reporting Requirements,'' and modify the bases for 
    Section 15.2.2, ``Safety Limit, Reactor Coolant System Pressure,'' and 
    Section 15.3.1.C, ``Maximum Coolant Activity,'' to incorporate changes 
    associated with the operation of Point Beach Nuclear Plant (PBNP), Unit 
    2, with replacement steam generators. The new analyses performed for 
    replacing Unit 2 steam generators resulted in changes to the reactor 
    core safety limits and protective instrumentation setpoints for Unit 1 
    as well as Unit 2. Calculations are based on operation at either 2000 
    psia or 2250 psia and an average temperature limit of greater than or 
    equal to 557 degrees Fahrenheit and less than or equal to 573.9 degrees 
    Fahrenheit. New dose calculations were performed based on new setpoints 
    for low-low steam generator water level, new values of primary and 
    secondary steam generator volumes, and revised accident analyses for 
    steam generator tube rupture, main steam line break, locked rotor, and 
    control rod ejection. Additional license conditions are proposed to 
    document the commitments made to improve habitability of the control 
    room so that dose limits do not exceed 10 CFR Part 50, Appendix A, 
    General Design Criterion 19, without relying on the use of potassium 
    iodide pills and/or self-contained breathing apparatus. The original 
    applications were previously noticed in the Federal Register on July 3, 
    1996 (61 FR 34903 and 34904).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed TS changes reflect the replacement of steam 
    generators at PBNP, including new analyses and setpoints, and a 
    different standard and acceptance criteria for Dose Equivalent I-
    131. The proposed setpoints maintain the margin to safe operation of 
    Unit 2 with the replacement steam generators. In order to maintain 
    one set of safety analyses for both units, the analyses for 
    operation of Unit 2 with the replacement steam generators were 
    performed to encompass the operation of Unit 1. Therefore, the 
    proposed changes apply to the operation of both units and maintain 
    the margin of safety for each. The staff independently performed an 
    evaluation of the dose consequences for steam generator tube 
    rupture, main steam line break, locked rotor accident, and a rod 
    ejection accident. The staff determined there are no significant 
    increases in dose for the low population zone or the exclusion area 
    boundary. The licensee had not previously analyzed these accidents 
    for control room habitability. As a result of the proposed changes, 
    limiting control room doses will require compensatory measures, use 
    of potassium iodide and self-contained breathing apparatus, which 
    have been previously approved, until such time that the control room 
    ventilation design is improved. The commitments to improve control 
    design/operation are included as license conditions. Therefore, the 
    proposed changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Installation of new steam generators, with a small increase in 
    primary side volume and new setpoints for instrumentation, does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated. The proposed setpoints
    
    [[Page 17244]]
    
    maintain the margin to safe operation of Unit 2 with the replacement 
    steam generators. In order to maintain one set of safety analyses 
    for both units, the analyses for operation of Unit 2 with the 
    replacement steam generators were performed to encompass the 
    operation of Unit 1. Therefore, the proposed changes apply to the 
    operation of both units and maintain the margin of safety for each. 
    These changes do not affect any of the parameters or conditions that 
    contribute to initiation of any accidents. Therefore, the proposed 
    changes will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        (3) The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed setpoints maintain the margin to safe operation of 
    Unit 2 with the replacement steam generators. In order to maintain 
    one set of safety analyses for both units, the analyses for 
    operation of Unit 2 with replacement steam generators were performed 
    to encompass the operation of Unit 1. Therefore, the proposed 
    changes apply to the operation of both units and maintain the margin 
    of safety for each. Compensatory measures will ensure control room 
    doses remain within the dose guidelines in 10 CFR Part 50, Appendix 
    A, General Design Criterion 19, until such time as the control 
    ventilation system design/operation is revised. Therefore, the 
    proposed changes do not involve a significant reduction in a margin 
    of safety.
        Based on this review, it appears that the three standards of 10 
    CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment requests involve no significant hazards 
    consideration.
    
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Power Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendment request: September 30, 1996, as supplemented 
    November 26, and December 12, 1996, February 13, and March 5, 1997 
    (TSCR 192).
        Description of amendment request: The proposed amendments would 
    revise License Nos. DPR-24 and DPR-27 to add commitments for control 
    room habitability and revise Technical Specification (TS) Sections 
    15.3.3, ``Emergency Core Cooling System, Auxiliary Cooling Systems, Air 
    Recirculation Fan Coolers, and Containment Spray,'' TS 15.3.7, 
    ``Auxiliary Electrical Systems,'' 15.5.2, ``Design Features-
    Containment,'' and associated TS Bases to reflect proposed changes to 
    the limiting conditions for operation, action statements, allowable 
    outage times, and design specifications for the Point Beach Nuclear 
    Plant (PBNP) TS associated with the containment accident fan coolers, 
    service water equipment (pumps and piping), component cooling water 
    pumps, and normal and emergency power supplies. Specifically, these 
    proposed changes increase the number of service water pumps and 
    component cooling water pumps required to be operable, change the 
    description of the service water system to define three separate loops, 
    modify the limiting conditions for operation of the containment cooling 
    and iodine removal systems and the component cooling water and service 
    water systems, modify the auxiliary electrical system requirements, 
    modify the associated TS Bases, and change the design value for each 
    containment ventilation/air coolers from 55,600 Btu/sec to 41,700 Btu/
    sec. The original application was previously noticed in the Federal 
    Register on November 19, 1996 (61 FR 58905).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes involve components currently installed in 
    the facilities and reflect current capabilities of this equipment. 
    Increasing the number of service water and component cooling water 
    pumps required to be operable, changing the service water header 
    definitions and modifying the limiting conditions for operation for 
    service water and component cooling water, and modifying the 
    requirements for the 4160/480-volt safeguards buses does not 
    increase the probabilities of any accidents currently evaluated in 
    the final safety analysis report (FSAR). The probabilities of 
    accidents previously evaluated in the FSAR are based on the 
    probability of initiating events for these accidents. Initiating 
    events for accidents previously evaluated for Point Beach include: 
    Control rod withdrawal and drop, CVCS [chemical volume and control 
    system] malfunction (boron dilution), startup of an inactive reactor 
    coolant loop, reduction in feedwater enthalpy, excessive load 
    increase, losses of reactor coolant flow, loss of external 
    electrical load, loss of normal feedwater, loss of all AC power to 
    the auxiliaries, turbine overspeed, fuel handling accidents, 
    accidental releases of waste liquid or gas, steam generator tube 
    rupture, steam pipe rupture, control rod ejection, and primary 
    coolant system ruptures. The change to the heat removal capability 
    of the containment ventilation/air coolers from 55,600 Btu/sec to 
    41,700 Btu/sec was evaluated to ensure that containment design is 
    not challenged. Therefore, the proposed changes do not affect the 
    probability of occurrence or the consequences of any accident 
    previously evaluated in the FSAR. During review of the proposed 
    changes, the staff determined that other changes made to the 
    operation of the containment spray system and the control room 
    ventilation design and operation could affect the doses associated 
    with a loss-of-coolant accident. The staff has determined that there 
    is no significant increase in offsite doses. As a result of the 
    proposed changes and current plant design, limiting control room 
    doses will require compensatory measures, use of potassium iodide 
    and self-contained breathing apparatus, which have been previously 
    approved, until such time that the control room ventilation design/
    operation is improved. The commitments to improve control design/
    operation are included as license conditions.
        (2) The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not introduce any new accidents from any 
    previously evaluated. Failures for the systems affected by the 
    proposed changes, service water system, component cooling water 
    system, containment ventilation/air cooling units, and the 4160/480-
    volt safeguards buses are factored into the accident analyses 
    included in the FSAR. No new or different kinds of accidents are 
    created since no new or different accident initiators or sequences 
    are involved. Therefore, these proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated in the Point Beach FSAR.
        (3) The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes provide the appropriate limiting conditions 
    for operation, action statements, allowable outage times, and design 
    specifications for service water, component cooling water, 
    containment cooling, and normal and emergency power supplies. This 
    ensures that the safety systems that protect the reactor and 
    containment will operate as required. The impact of changes to 
    design and operation of affected systems do not affect the reactor 
    and containment design. Therefore, the margins of safety for Point 
    Beach are not being reduced because the design and operation of the 
    reactor and containment are not being changed and the safety systems 
    and limiting conditions of operation for these safety systems that 
    provide their protection that are being changed will continue to 
    meet the requirements for accident mitigation for PBNP. Compensatory 
    measures will ensure control room doses remain within the dose 
    guidelines in 10 CFR Part 50, Appendix A, General Design Criterion 
    19, until such time as the control ventilation system design/
    
    [[Page 17245]]
    
     operation is revised. Therefore, the proposed changes will not 
    create a significant reduction in a margin of safety.
    
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment requests involve no significant hazards 
    consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: March 7, 1997.
        Description of amendment request: The proposed amendments would 
    revise Technical Specification 3/4.7.1.6 and Section 15.6.3 of the 
    Updated Final Safety Analysis Report to require four instead of three 
    steam generator pressure operated relief valves operable.
        Date of publication of individual notice in Federal Register: March 
    13, 1997 (62 FR 11931).
        Expiration date of individual notice: April 14, 1997.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
     Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: March 17, 1997.
        Brief description of amendment request: The proposed amendment 
    would modify the Design Features Section 5.3.1 of the Technical 
    Specifications to reflect the Atrium-10 design and would include a 
    Siemens Power Corporation topical report reference in Section 6.9.3.2 
    to reflect mechanical design criteria for this fuel. This change would 
    allow this fuel to be loaded and maintained in the core only under 
    Condition 5, (refueling).
        Date of publication of individual notice in Federal Register: March 
    25, 1996 (62 FR 14167).
        Expiration date of individual notice: April 24, 1997.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) The 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units 1, 2, 
    and 3, Maricopa County, Arizona
    
        Date of application for amendments: May 2, 1995, as supplemented by 
    letter dated March 7, 1996.
        Brief description of amendments: These amendments modify the 
    licenses to authorize incorporation in the Updated Final Safety 
    Analysis Report (UFSAR) of certain changes to the description of the 
    facilities involving a revised large-break loss of coolant accident 
    (LOCA) analysis that addresses a previously unanalyzed release path 
    through the steam generators to the atmosphere.
        Date of issuance: March 17, 1997.
        Effective date: March 17, 1997, to be implemented within 60 days of 
    issuance.
        Amendment Nos.: Unit 1--111; Unit 2--103; Unit 3--83.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Operating Licenses and Updated Final Safety 
    Analysis Report.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62487). The March 7, 1996, supplemental letter provided additional 
    clarifying information and did not change the initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    March 17, 1997. No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: January 29, 1997, as 
    supplemented February 6, and February 21, 1997.
        Brief description of amendment: The amendment adds a new Technical
    
    [[Page 17246]]
    
    Specification 3.0.5 to provide guidance for returning equipment to 
    service under administrative controls for the sole purpose of 
    performing testing to demonstrate operability.
        Date of issuance: March 17, 1997.
        Effective date: March 17, 1997.
        Amendment No.: 69.
        Facility Operating License No. NPF-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 
    (62FR6569).
        The February 6, and February 21, 1997 letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 17, 1997.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: January 10, 1997, as 
    supplemented January 31, February 20, and March 3, 1997.
        Brief description of amendment: The amendment revises Technical 
    Specification 4.8.1.1.2 to clarify pressure testing requirements for 
    the isolable and non-isolable portions of the diesel fuel oil piping.
        Date of issuance: March 19, 1997.
        Effective date: March 19, 1997.
        Amendment No.: 70.
        Facility Operating License No. NPF-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 5, 1997 (62 FR 
    5490). The January 31, February 20, and March 3, 1997, letters provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 19, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina.
    
        Date of application for amendments: November 4, 1996 and 
    supplemented February 5, 1997.
        Brief description of amendments: The amendments revise Technical 
    Specification Section 4.7.13.1.c to eliminate the requirement that the 
    18-month Standby Shutdown System diesel generator inspection be 
    performed only during shutdown of both reactors.
        Date of issuance: March 13, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1--157--Unit 2--149.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64383) The supplemental letter dated February 5, 1997, provided 
    additional information that did not change the scope of the November 4, 
    1996, application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 13, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: January 13, 1997.
        Brief description of amendments: The amendments revise the 
    Technical Specifications so that the containment integrated leak rate 
    Type A testing will now be performed consistent with the revised 10 CFR 
    Part 50, Appendix J, Option B, by referring to Regulatory Guide 1.163, 
    ``Performance-Based Containment Leak-Test Program.'' No changes to 
    implement Option B for the Type B and Type C tests were requested by 
    the licensee at this time.
        Date of issuance: March 21, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: Unit 1--173--Unit 2--155.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6575) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 21, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, North Carolina 28223-0001.
    
    Duke Power Company, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: February 15, 1996, as 
    supplemented by letter dated February 18, 1997.
        Brief description of amendments: The amendments add operability and 
    surveillance requirements regarding operation and testing of the Keowee 
    Hydro Station to the Oconee Technical Specifications.
        Date of Issuance: March 20, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days. Implementation shall include revision of the Selected Licensee 
    Commitment manual to incorporate the Keowee Hydro units' commercial 
    power operating restrictions curves in accordance with the application 
    for the amendments.
        Amendment Nos.: Unit 1--222; Unit 2--222; Unit 3--219.
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: March 27, 1996 (61 FR 
    13523) The February 18, 1997, letter provided clarifying information 
    that did not change the scope of the February 15, 1996, application and 
    the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 20, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691.
    
    [[Page 17247]]
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of application for amendments: September 18, 1992, as 
    supplemented October 6, 8, 15, 23, and November 13 and 20, 1992, March 
    5, May 24, June 10, and December 20, 1993, April 6 and July 28, 1995, 
    and September 11, October 1, December 13, 19 and 23, 1996.
        Brief description of amendments: The amendments modify the Facility 
    Operating Licenses, Technical Specifications, Environmental Protection 
    Plan, and Antitrust conditions to add Southern Nuclear Operating 
    Company, Inc., as operator of the facilities, with exclusive 
    responsibility and control over its physical construction, operation, 
    and maintenance. The antitrust license conditions divorce Southern 
    Nuclear from marketing or brokering power or energy from the Hatch 
    Plant and holds Georgia Power Company accountable for the actions of 
    its agent, Southern Nuclear, to the extent Southern Nuclear's actions 
    contravene the Hatch antitrust license conditions. An Order Approving 
    Southern Nuclear Operating Company, Incorporated, As Exclusive Operator 
    was included along with the issuance of the amendments.
        Date of issuance: March 17, 1997.
        Effective date: To be implemented within 60 days of the date of 
    issuance.
        Amendment Nos.: 203 and 144.
        Facility Operating License Nos. DPR-57 and NPF-5: Amendments 
    revised the Technical Specifications and Operating Licenses.
        Date of initial notice in Federal Register: October 14, 1992 (57 FR 
    47131). The October 6, 8, 15, 23, and November 13 and 20, 1992, March 
    5, May 24, June 10, and December 20, 1993, April 6 and July 28, 1995, 
    and September 11, October 1, December 13, 19 and 23, 1996, letters, did 
    not change the scope of the September 18, 1992, application and the 
    initial proposed no significant hazards consideration determination. 
    The Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated March 17, 1997, and an Environmental Assessment 
    dated October 27, 1992.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of application for amendments: October 7, 1996.
        Brief description of amendments: The amendments revise Surveillance 
    Requirements (SRs) 3.1.7.7 and 3.4.3.1, and Limiting Conditions for 
    Operation 3.4.3, 3.5.1, and 3.6.1.6 to increase the nominal mechanical 
    pressure relief setpoints for all of the 11 safety/relief valves (SRVs) 
    to 1150 psig and allow operation with one SRV and its associated 
    functions inoperable. The change will reduce the potential for SRV 
    pilot leakage and the potential for forced outages due to an inoperable 
    SRV during a fuel cycle.
        Date of issuance: March 21, 1997.
        Effective date: As of the date of issuance to be implemented for 
    Unit 1 prior to startup from its refueling outage scheduled for fall 
    1997; and for Unit 2 prior to startup from its refueling outage 
    currently scheduled for March 15, 1997.
        Amendment Nos.: 204 and 145.
        Facility Operating License Nos. DPR-57 and NPF-5: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 2, 1997 (62 FR 
    129). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 21, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of application for amendments: October 29, 1996, as 
    supplemented February 19, 1997.
        Brief description of amendments: The amendments revise the 
    Technical Specifications associated with the installation of a digital 
    Power Range Neutron Monitoring system.
        Date of issuance: March 21, 1997.
        Effective date: As of the date of issuance to be implemented for 
    Unit 1 prior to its startup from the fall of 1997 refueling outage; and 
    implemented for Unit 2 prior to its startup from the spring of 1997 
    refueling outage.
        Amendment Nos.: 205 and 146.
        Facility Operating License Nos. DPR-57 and NPF-5: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 2, 1997 (62 FR 
    130). The February 19, 1997, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 21, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear
    
        Date of application for amendment: November 27, 1996 (TSCR 232).
        Brief description of amendment: The amendment changes the 
    acceptance criteria for the individual cell voltage from 2.0v to 2.09v, 
    the frequency for battery specific gravities to implement the 
    recommendations of IEEE 450-1995, deletes surveillance 4.7.B.4.d, and 
    adds a clarifing phrase ``while on a float charge . . .'' where 
    appropriate.
        Date of Issuance: March 24, 1997.
        Effective date: March 24, 1997.
        Amendment No.: 189.
        Facility Operating License No. DPR-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6576) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated March 24, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: November 20, 1996, as supplemented by 
    letters dated February 20, 1997, and March 25, 1997.
        Brief description of amendment: The amendment revises Section 5.2 
    of the Fort Calhoun Station technical specifications to relocate 
    controls for working hours to the Updated Safety Analysis Report.
        Date of issuance: March 27, 1997.
        Effective date: March 27, 1997.
        Amendment No.: 181.
    
    [[Page 17248]]
    
        Facility Operating License No. DPR-40: Amendment revised the 
    Technical Specifications and operating license.
        Date of initial notice in Federal Register: January 2, 1997 (62 FR 
    131) The February 20, 1997, and March 25, 1997, supplemental letters 
    provided additional clarifying information that did not change the 
    portion of the initial no significant hazards consideration 
    determination that addressed this proposed change.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 27, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: January 11, 1996, as 
    supplemented by letters dated February 26, May 22, June 27, July 12, 
    December 23, 1996, and March 17, 1997
        Brief description of amendment: The amendments revise Section 6.0 
    (Administrative Controls) of the Hope Creek TS to: (1) Relocate the 
    requirements of Section 6.5 (Station Operations Review Committee, 
    Nuclear Safety Review and Audit, and Technical Review and Control) to 
    the Quality Assurance Program, (2) replace specific management titles 
    with generic management functional positions, (3) change Operating 
    Engineer to Assistant Operations Manager, (4) require a Senior Reactor 
    Operator license be held by either the Operations Manager or one of the 
    Assistant Operations Managers, and (5) correct some typographical 
    errors in Section 6.0.
        Date of issuance: March 21, 1997.
        Effective date: As of date of issuance and shall be implemented 
    within 60 days.
        Amendment No.: 97.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications and the license.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5817).
        The supplemental letters provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination nor the original notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated March 21, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: October 25, 1996, as 
    supplemented by letters dated December 4, 1996, and January 24, 1997.
        Brief description of amendment: This amendment changes Hope Creek 
    Technical Specification (TS) 3/4.1.3.5, ``Control Rod Scram 
    Accumulator,'' in order to: 1) Permit a separate entry into a TS action 
    statement for each inoperable control rod; 2) provide more specific 
    applicability for required actions in Operational Condition 1 or 2 with 
    one inoperable control rod scram accumulator (reactor pressure of 
     900 psig would be specified); 3) provide more specific 
    actions (verify charging water pressure) for two or more inoperable 
    control rod scram accumulators when reactor pressure is  900 
    psig; 4) provide more specific actions when reactor pressure is < 900="" psig="" and="" one="" or="" more="" control="" rod="" scram="" accumulators="" are="" inoperable="" (verify="" insertion="" of="" control="" rods="" associated="" with="" inoperable="" accumulators="" and="" verify="" that="" charging="" water="" header="" pressure="" is=""> 940 psig); 5) provide specific actions in Operational 
    Condition 5 with one or more withdrawn control rods inoperable; and 6) 
    eliminate the requirements to perform an 18-month channel functional 
    test of the leak detectors and the 18-month channel calibration of the 
    pressure detectors.
        Date of issuance: March 26, 1997.
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment No.: 98.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64394) The December 4, 1996, and January 24, 1997, supplements did not 
    change the initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 26, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: January 11, 1996, as 
    supplemented by letters dated February 26, May 22, June 27, July 12, 
    December 23, 1996, and March 17, 1997.
        Brief description of amendments: The amendments revise Section 6.0 
    (Administrative Controls) of the Salem TS to: 1) relocate the 
    requirements of Section 6.5 (Station Operations Review Committee, 
    Nuclear Safety Review and Audit, and Technical Review and Control) to 
    the Quality Assurance Program, 2) replace specific management titles 
    with generic management functional positions, 3) change Operating 
    Engineer to Assistant Operations Manager, 4) require a Senior Reactor 
    Operator license be held by either the Operations Manager or one of the 
    Assistant Operations Managers, and 5) correct some typographical errors 
    in Section 6.0.
        Date of issuance: March 21, 1997.
        Effective date: Both units, as of date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 192 and 175.
        Facility Operating License Nos. DPR-70 and DPR-75: The amendments 
    revised the Technical Specifications and the license.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5818) The supplemental letters provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination nor the original notice.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 21, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 Joseph 
    M. Farley Nuclear Plant, Unit 1, Houston County, Alabama
    
        Date of amendment request: December 26, 1997, as supplemented by 
    letter dated February 6, March 7, and March 21, 1997.
        Brief Description of amendment: The amendment changes Technical 
    Specification 3/4.4.6, ``Steam Generators'' and associated Bases to 
    implement the voltage-based alternate repair criteria for steam 
    generator tubes in Farley Unit 1 in accordance with
    
    [[Page 17249]]
    
    Generic Letter 95-05, ``Voltage-Based Repair Criteria for Westinghouse 
    Steam Generator Tubes Affected by Outside Diameter Stress Corrosion 
    Cracking.''
        Date of issuance: March 24, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 124.
        Facility Operating License Nos. NPF-2 and NPF-8: Amendment revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4353) By letter dated February 6, 1997, the licensee submitted 
    additional information to clarify the changes to the proposed repair 
    criteria, which did not change the scope of the December 26, 1996, 
    application and the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated March 24, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama
    
        Date of amendments request: January 10, 1997, as supplemented by 
    letter dated February 24, 1997.
        Brief Description of amendments: The amendments revise the 
    Technical Specifications (TS) to incorporate the latest revised topical 
    reports governing the installation of laser welded steam generator tube 
    sleeves. In addition, the reference to a one-cycle implementation of 
    L*, which expired at the last Unit 2 outage was deleted from the Unit 2 
    TS.
        Date of issuance: March 24, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 125 and 119.
        Facility Operating License Nos. NPF-2 and NPF-8: Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4355) The February 24, 1997, letter provided clarifying information 
    that did not change the original application and the initial proposed 
    no significant hazards consideration determination published in the 
    Federal Register on January 29, 1997 (62 FR 4355).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated March 24, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
    364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, 
    Alabama
    
        Date of amendments request: September 30, 1996.
        Brief description of amendments: The amendments revise Technical 
    Specifications (TS) 3/4.1.1.1, 3/4.1.1.2, 3/4.1.1.3, 3/4.1.3.5, 
    3.1.3.6, 3.2.1, 3.2.2 and 3.2.3 and associated Bases to remove certain 
    cycle-specific parameter limits from the TS and relocate them to the 
    Core Operating Limits Report.
        Date of issuance: March 25, 1997.
        Effective date: As of the date of issuance to be implemented for 
    Unit 1 prior to entry into Mode 5 following the next scheduled 
    refueling outage, which should begin in March 1997; for Unit 2 prior to 
    entry into Mode 5 following the refueling outage scheduled to begin in 
    March 1998.
        Amendment Nos.: 126 and 120.
        Facility Operating License Nos. NPF-2 and NPF-8: Amendments revise 
    the Technical Specifications and License Conditions.
        Date of initial notice in Federal Register: November 6, 1996 (61 FR 
    57491) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated March 25, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
    
    Southern California Edison Company, et al., Docket No. 50-362, San 
    Onofre Nuclear Generating Station, Unit No. 3, San Diego County, 
    California
    
        Date of application for amendment: February 18, 1997, as 
    supplemented by letter dated February 21, 1997.
        Brief description of amendment: The amendment defers implementation 
    of Surveillance Requirement 3.3.5.6 of Technical Specifcation 3.3.5, 
    ``Engineered Safety Features Actuation System (ESFAS) 
    Instrumentation,'' until the next SONGS Unit 3 shutdown, which will be 
    no later than the upcoming Cycle 9 refueling outage (currently 
    scheduled for April 12, 1997).
        Date of issuance: March 17, 1997.
        Effective date: March 17, 1997.
        Amendment No.: 127
        Facility Operating License No. NPF-15: The amendments revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes (62 FR 9001 dated February 27, 1997). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by March 31, 1997, but indicated that if the Commission makes a 
    final no significant hazards consideration determination any such 
    hearing would take place after issuance of the amendment. The February 
    21, 1997, letter provided additional clarifying information and did not 
    change the original no significant hazards consideration determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated March 17, 1997.
        Attorney for licensee: Douglas K. Porter, Esquire, Southern 
    California Edison Company, P. O. Box 800, Rosemead, California 91770.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: February 14, 1997.
        Brief description of amendment: This amendment revises Technical 
    Specification (TS) Section 3/4.5.2, ``Emergency Core Cooling Systems, 
    ECCS Subsystems--Tavg  280 deg.F.'' Surveillance 
    requirement 4.5.2.f would be modified to state that opening and closing 
    of the inspection port on the watertight enclosure for the decay heat 
    valve pit would not require this surveillance procedure to be 
    performed. This amendment also revises the applicable TS bases.
        Date of issuance: March 24, 1997.
        Effective date: Immediately, and shall be implemented no later than 
    120 days after issuance.
        Amendment No.: 215.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration (NSHC): Yes (62 FR 8783 dated February 26, 1997). The 
    notice
    
    [[Page 17250]]
    
    provided an opportunity to submit comments on the Commission's proposed 
    NSHC determination. No comments have been received. The notice also 
    provided for an opportunity to request a hearing by March 30, 1997, but 
    indicated that if the Commission makes a final NSHC determination, any 
    such hearing would take place after issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final determination of NSHC are contained in 
    a Safety Evaluation dated March 24, 1997.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, Ohio 43606.
    
    United States Department of Commerce, National Institute of Standards 
    and Technology, Docket No. 50-184, NIST Test Reactor
    
        Date of application for amendment: January 17, 1997.
        Brief description of amendment: This amendment revises the 
    Technical Specifications to change the name of the Reactor Radiation 
    Division to the NIST Center for Neutron Research and the Chief, 
    Radiation Division to Director, NIST Center for Neutron Research.
    
        Date of issuance: March 31, 1997.
        Effective date: March 31, 1997.
        Amendment No.: 8.
        Amended Facility License No. TR-5: This amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8801). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated March 31, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room Location: N/A.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) The 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By May 9, 1997, the licensee 
    may file a request for a hearing with respect to issuance of the 
    amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the
    
    [[Page 17251]]
    
    designated Atomic Safety and Licensing Board will issue a notice of a 
    hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: December 27, 1996, as 
    supplemented by letter dated March 18, 1997.
        Brief description of amendments: The amendments modify the licenses 
    to authorize incorporation of certain changes to the description of the 
    facilities involving offsite power sources into the Updated Final 
    Safety Analysis Report (UFSAR) for the Palo Verde Nuclear Generating 
    Station (PVNGS).
        Date of issuance: March 26, 1997.
        Effective date: March 26, 1997, to be implemented within 60 days of 
    the date of issuance.
        Amendment Nos.: Unit 1--112; Unit 2--104; Unit 3--84.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the operating licenses and the Updated Final Safety 
    Analysis Report.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated March 
    26, 1997.
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004.
        NRC Project Director: William H. Bateman.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: March 26, 1997, as supplemented 
    on March 27, 1997.
        Brief description of amendments: The proposed amendments provided 
    (1) An evaluation of the Unreviewed Safety Question (USQ) involving the 
    control room operator dose resulting from error in the secondary 
    containment volume, (2) a change in Technical Specification (TS) 
    4.7.P.2.b and 4.7.P.3 values for the allowed methyl iodide penetration 
    for the standby gas treatment charcoal adsorbers, and (3) change of TS 
    5.2.C to reflect the new calculated free volume of the secondary 
    containment.
        Date of Issuance: March 27, 1997.
        Effective date: March 27, 1997.
        Amendment Nos.: 175, 171.
        Facility Operating License Nos. DPR-29 and DPR-30: The amendments 
    revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendments, finding of 
    emergency circumstances and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated March 
    27, 1997.
    
    [[Page 17252]]
    
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
        NRC Project Director: Robert A. Capra.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue County, 
    Minnesota
    
        Date of application for amendments: January 29, 1997, as 
    supplemented February 11, 12, March 7, 10, 11, 19, and 20, 1997.
        Brief description of amendments: The amendments authorize Northern 
    States Power Company to continue operation of Prairie Island Units 1 
    and 2 on an interim basis, through the incorporation of three license 
    conditions into its licenses, until a seismically qualified emergency 
    cooling water source is provided that will provide the basis to extend 
    the time for operator post-seismic cooling water load management. This 
    could be done either through a seismic evaluation of the intake canal, 
    physical modifications to the intake canal or plant, or some 
    combination of the two.
        Date of issuance: March 25, 1997.
        Effective date: March 25, 1997, with implementation of License 
    Condition 1 prior to Unit 2 entering Mode 2, with implementation of the 
    requirements of License Condition 2 by July 1, 1997, and December 31, 
    1998, and with implementation of License Condition 3 at the next 
    updated safety analysis report update following completion of License 
    Condition 2, but no later than June 1, 1999.
        Amendment Nos.: 128 and 120.
        Facility Operating License Nos. DPR-42 and DPR-60: Amendments 
    revised the licenses.
        Public comments requested as to proposed no significant hazards 
    consideration (NSHC): Yes (62 FR 5857 dated February 7, 1997). This 
    notice provided an opportunity to submit comments on the Commission's 
    proposed NSHC determination. The notice also provided for an 
    opportunity to request a hearing by March 10, 1997, but indicated that 
    if the Commission makes a final NSHC determination, any such hearing 
    would take place after issuance of the amendments. Because of the 
    significant revisions to the licensee's original application, NRC also 
    published a public notice of the proposed amendments, issued a proposed 
    finding of no significant hazards consideration, and requested that any 
    comments on the proposed finding be provided to the staff by close of 
    business on March 20, 1997. The notice was published in the St. Paul 
    Pioneer Press on March 15, 1997, the Minneapolis Star Tribune on March 
    16, 1997, and the Red Wing Republican Eagle on March 17, 1997. No 
    comments have been received. The Commission's related evaluation of the 
    amendments, finding of exigent circumstances, and final determination 
    of NSHC are contained in a Safety Evaluation dated March 25, 1997.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        NRC Project Director: John N. Hannon.
    
        Dated at Rockville, Maryland, this 2nd day of April, 1997.
    
        For the Nuclear Regulatory Commission.
    Jack W. Roe,
    Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 97-8916 Filed 4-8-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
04/09/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-8916
Dates:
March 17, 1997, to be implemented within 60 days of issuance.
Pages:
17223-17252 (30 pages)
PDF File:
97-8916.pdf