94-11226. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 91 (Thursday, May 12, 1994)]
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    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 94-11226]
    
    
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    [Federal Register: May 12, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
     
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from April 18, 1994, through April 29, 1994. The 
    last biweekly notice was published on April 28, 1994 (59 FR 22000).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11555 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By June 10, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of amendment request: March 30, 1994.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3/4.4.9, Pressure/Temperature 
    Limits, and its associated Bases, by changing the Unit 1 heatup and 
    cooldown curves to incorporate a newly determined reactor vessel 
    reference nil-ductility temperature, RTNDT, and by updating the 
    removal schedule of vessel surveillance capsules for both units in 
    accordance with ASTM E185-82. Changes would also be made to the Unit 1 
    Low Temperature Overpressure Protection System (LTOPS) setpoint curve 
    in TS 3.4.9.3 to reflect the new pressure/temperature limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The use of new pressure-temperature limit curves and low 
    temperature overpressure protection curves will not change any 
    postulated accident scenarios. The revised curves were developed using 
    industry standards and regulations which are recognized as being 
    inherently conservative. The pressure-temperature low temperature 
    overpressure curves provide reactor coolant system (RCS) limits to 
    protect the reactor pressure vessel from brittle fracture by clearly 
    separating the region of normal operations from the region where the 
    vessel is subject to brittle fracture. The heatup and cooldown limits 
    are designed to ensure that the 10 CFR 50 Appendix G Pressure 
    Temperature limits for the RCS are not exceeded during any condition of 
    normal operation including anticipated operational occurrences.
        General Design Criterion 32 of 10 CFR 50 Appendix A requires that 
    the reactor coolant boundary shall be designed with sufficient margin 
    to assure that when stressed under operating, maintenance, testing, and 
    postulated accident condition[s], (1) the boundary behaves in a 
    nonbrittle manner and (2) the probability of rapidly propagating 
    fracture is minimized.
        10 CFR 50 Appendix G, ``Fracture Toughness Requirements,'' requires 
    that the effects of changes in the fracture toughness of reactor vessel 
    materials caused by neutron radiation throughout the service life of 
    [a] nuclear reactor be considered in the pressure-temperature limits. 
    The change is used in conjunction with the material initial reference 
    temperature (RTNDT) to establish the limiting pressure-temperature 
    curves. Regulatory Guide 1.99, Rev. 2, contains procedures for 
    calculating the effects of neutron radiation embrittlement of the low-
    alloy steels currently used for light-water-cooled reactor vessels.
        Using the Regulatory Guide 1.99, Revision 2, Braidwood Unit 1 
    Surveillance Capsule U results, and Appendix G to 10 CFR 50, new 
    Pressure-Temperature curves [were] prepared for the projected reactor 
    vessel exposure at 32 EFPY of operation. These new curves, in 
    conjunction with the heatup and cooldown ranges and the revised Low-
    Temperature Overpressure Protection System setpoints, provide the 
    required assurance that the reactor pressure vessel is protected from 
    brittle fracture up 32 EFPY of operation. No changes to the design of 
    the facility have been made and no new equipment has been added or 
    removed. The revised analysis and resultant adjustment of the operating 
    limitations provide assurance that the Reactor Coolant System is 
    protected from brittle fracture.
        Revising the Reactor Vessel Material Surveillance Program 
    Withdrawal Schedule does not result in the addition or removal of any 
    equipment, or any design changes to the facility. Capsule lead times 
    are revised and, for Braidwood Unit 2, Capsule X will be removed next 
    vice Capsule W. The proposed removal schedules remain consistent with 
    ASTM 185-82.
        Therefore, the proposed amendment to the pressure temperature 
    limitations does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        B. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The use of the new pressure-temperature operating limits and the 
    new low temperature overpressure protection curve does not change any 
    postulated accident scenarios. The new curves do not represent any 
    appreciable change in the current methodologies; they merely provide 
    assurance that the Reactor Coolant System is protected from brittle 
    fracture. No new accident or malfunction mechanism is introduced by the 
    amendment and no physical plant changes will result from this 
    amendment.
        Revision of the Reactor Vessel Material Surveillance Program 
    Withdrawal Schedule does not introduce a new accident or malfunction 
    mechanism. Capsule lead times are revised, and, other than changing the 
    order of specimen removal, consistent with ASME 185-82, no physical 
    plant changes will result from this revised schedule.
        Therefore, the proposed changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        C. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The new pressure-temperature operating limits low temperature 
    overpressure protection curves were generated with the currently 
    accepted conservative methodology using capsule surveillance data. The 
    new pressure-temperature curves were developed using industry standards 
    and regulations (ASME Code Section III, and NRC Regulatory Guide 1.99, 
    Revision 2) which are recognized as being inherently conservative. The 
    use of the new pressure- temperature operating limits and low 
    temperature overpressure protection limits would not change postulated 
    accident scenarios.
        The proposed revision to the Reactor Vessel Material Surveillance 
    Program Withdrawal Schedule would not change postulated accident 
    scenarios. Capsule lead times are revised, and, other than changing the 
    order of specimen removal, consistent with ASTM 185- 82, no physical 
    plant changes will result from this revised schedule. Therefore, the 
    proposed changes do not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Wilmington Township Public 
    Library, 201 S. Kankakee Street, Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: James E. Dyer.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: March 31, 1994.
        Description of amendment request: The proposed amendment would 
    change the Technical Specifications (TS) to provide allowable outage 
    times for automatic actuation channel surveillance testing and 
    restoration time for an inoperable engineered safety feature actuation 
    system automatic actuation channel.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The following evaluation is provided for the three categories of 
    the significant hazards consideration standards:
        a. Proposed changes to allow 8 hours for master relay and logic 
    testing, 12 hours for slave relay testing and 6 hours to restore an 
    inoperable ESFAS Automatic Actuation Channel prior to entering the 
    shutdown action clock.
        (1) The determination that these changes are within all acceptable 
    criteria was established in the NRC's SER prepared for WCAP-10271, 
    Supplement 2, Revision 1. The Technical Specification changes proposed 
    by this license amendment request conform to NRC guidance contained in 
    the SER. The NRC found that implementation of the proposed changes is 
    expected to result in a small and acceptable increase in ESFAS 
    unavailability. This increase in probability results in a small 
    increase in calculated core damage frequency and public risk. The 
    calculated increase in core damage frequency was judged to be 
    acceptable since the increase was small and well within the range of 
    uncertainty associated with the analysis. The values presented in WCAP-
    10271 Supplement 2 Revision 1 for increase in core damage frequency 
    were verified by Brookhaven National Laboratory as part of an audit and 
    sensitivity analyses performed for the NRC Staff.
        Based on the small increase in core damage frequency as compared 
    with the range of uncertainty in the analysis, the NRC agreed that the 
    calculated increase is acceptable. This conclusion was documented in 
    the NRC's SER dated February 22, 1989. The applicability of these 
    conclusions has been verified through a plant specific review of the 
    generic analysis in WCAP-10271, Supplement 2, Revision 1. The ESFAS 
    Automatic Actuation Channel allowed outage and restoration times 
    included in this license amendment request are consistent with the 
    generic analysis. In addition, the NRC stated that the majority of the 
    increase in unavailability was due to the decrease in frequency of 
    surveillance testing vice the changes in allowed outage and restoration 
    times. Therefore, considering the above information, the proposed 
    allowed outage and restoration time changes do not involve a 
    significant increase in the probability of occurrence or consequences 
    of an accident previously evaluated.
        (2) The proposed changes do not involve the physical alteration of 
    any plant system and do not result in a change in the manner in which 
    the ESFAS system performs its function. The increases in allowed outage 
    and restoration times only affects the probability of the ESFAS 
    Automatic Actuation Channel functioning properly as described above. 
    Therefore, the allowed outage and restoration time changes proposed in 
    this license amendment request do not create a new or different type of 
    accident from any previously evaluated.
        (3) The proposed allowed outage time and restoration time changes 
    do not alter the manner in which safety limits, limiting safety system 
    setpoints or limiting conditions for operation are determined. The 
    impact of the revised ESFAS Automatic Actuation Channel allowed outage 
    and restoration times is addressed above. Implementation of the 
    proposed changes is expected to result in an overall improvement in 
    safety by allowing adequate time for required ESFAS testing and quality 
    repairs leading to improved equipment reliability due to a more 
    appropriate restoration time. Therefore, it may be concluded that the 
    proposed allowed outage and restoration time changes do not involve a 
    significant reduction in margin of safety.
        b. Proposed change to the minimum required degree of redundancy for 
    the High-High Containment Pressure channels in Table 3.4-1.
        (1) Changing the minimum required degree of redundancy in Table 
    3.4-1 for the High-High Containment Pressure Channels (Table 3.4-1 
    items II.3, III.B.3, and IV.3) provides consistency with Technical 
    Specification 3.4.2.c which allows an inoperable High-High Containment 
    Pressure channel to be placed in bypass. Placement of an inoperable 
    High-High Containment Pressure Channel in bypass is preferred to reduce 
    the probability of an inadvertent containment spray event. Also, these 
    channels are designed with a two out of four logic so that the failed 
    channel may be bypassed rather than tripped. With the failed channel 
    bypassed, single failure criterion is still met because the logic is 
    now a two out of three. Furthermore, with the one channel bypassed, a 
    single channel failure will not inadvertently initiate a containment 
    spray. Therefore, this change can be considered an administrative 
    change to correct Table 3.4-1 to agree with the Action requirements of 
    Technical Specification 3.4.2.c. As such this proposed change does not 
    involve an increase in the probability of occurrence or consequences of 
    an accident previously evaluated.
        (2) Correcting the minimum required degree of redundancy in Table 
    3.4-1 for the High-High Containment Pressure channels is an 
    administrative change which does not involve the physical alteration of 
    any plant system and does not result in a change in the manner in which 
    the ESFAS system performs its function. Therefore, the proposed 
    correction to Table 3.4-1 does not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        (3) Correcting the minimum required degree of redundancy in Table 
    3.4-1 to be consistent with the Actions of Technical Specification 
    3.4.2.c is an administrative change and as such does not involve any 
    reduction in a margin of safety.
        c. Proposed change to the delete footnote +++ from Table 3.4-1.
        (1) Deleting footnote +++ from Table 3.4-1 removes the 
    inconsistency between it and Technical Specification 3.4.2.c which 
    states that channels other than the High-High Containment Pressure 
    channels shall be placed in trip during testing. The change does not 
    affect the manner in which ESFAS provides plant protection. In addition 
    the change does not affect the functioning of ESFAS or the way Zion 
    Station conducts channel testing. Instrument channel testing will 
    continue to be conducted in the tripped mode with the exception of the 
    High-High Containment Pressure channels, which can be tested in bypass 
    because of the risk of a spurious Containment Spray event. Automatic 
    Actuation Channel testing will be performed in accordance with the 
    allowed outage times of new Specification 3.4.2.d. As such this 
    proposed change does not involve any significant increase in the 
    probability of occurrence or consequences of an accident previously 
    evaluated.
        (2) Deleting footnote +++ from Table 3.4-1 does not involve the 
    physical alteration of any plant system and does not result in a change 
    in the manner in which ESFAS performs its function. Therefore this 
    change does not involve the physical alteration of any plant system and 
    does not result in a change in the manner in which the ESFAS system 
    performs its function. Therefore, the proposed correction to Table 3.4-
    1 does not create the possibility of a new or different kind of 
    accident from any previously analyzed.
        (3) Deleting footnote +++ from Table 3.4-1 does not alter the 
    manner in which safety limits, limiting safety system setpoints or 
    limiting conditions for operation are determined. Implementation of 
    this change will not alter ESFAS testing. Therefore implementation of 
    this change does not involve any reduction in a margin of safety.
        d. Proposed editorial change to Technical Specification 3.4.2.c.
        The editorial change to Technical Specification 3.4.2.c to change 
    ``Containment Hi-Hi pressure channels'' to ``High-High Containment 
    Pressure channels'' is purely an administrative change which has no 
    affect on plant safety.
        e. Summary.
        The foregoing analyses demonstrate that the proposed License 
    Amendment to the Zion Station Technical Specifications does not involve 
    a significant increase in the probability of occurrence or consequences 
    of a previously evaluated accident, does not create the possibility of 
    a new or different kind of accident and does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: James E. Dyer.
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of amendment request: April 22, 1994.
        Description of amendment request: The proposed change revises the 
    reactor vessel pressure-temperature limits in the Technical 
    Specifications. The change insures that the vessel fracture toughness 
    requirements of Section V of 10 CFR Part 50, Appendix G, are satisfied 
    through the end of life.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will the proposed change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The margin above Nil Ductility Transition Temperature (NDTT) is 
    governed by 10 CFR 50 Appendix G and remains unchanged. The proposed 
    change will not involve a significant increase in the probability or 
    consequences of a previously evaluated accident.
        2. Will the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The predicted shifts in NDTT are based on a revised reference 
    temperature consistent with Regulatory Guide 1.99, Revision 2, dated 
    May 1988. This method of revising temperature-pressure limits is the 
    same as in the past (ASME Code Section III, Appendix G).
        3. Will the proposed change involve a significant reduction in the 
    margin of safety?
        The proposed curves were generated for an End of Licensed Life (May 
    31, 2000) Effective Full Power Year exposure and are conservative in 
    nature until that time. The margin of safety [is] unchanged.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201.
        NRC Project Director: L. B. Marsh.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket No. 
    50-461, Clinton Power Station, Unit No. 1, DeWitt County, Illinois
    
        Date of amendment request: April 18, 1994.
        Description of amendment request: License Amendment No. 81, issued 
    on July 15, 1993, changed the numbering of surveillance requirements 
    for Technical Specifications 3/4.3.1, ``Control Rod Operability,'' 3/
    4.3.2, ``Control Rod Maximum Scram,'' and 3/4.10.2, ``Rod Pattern 
    Control System.'' However, Action Statements referencing these 
    surveillance requirements were overlooked and were not appropriately 
    renumbered. The purpose of the proposed technical specification change 
    would be to renumber the overlooked references.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        (1) These changes do not affect the intent or implementation of the 
    applicable Technical Specifications. The changes simply make the 
    affected Technical Specifications consistent. Since these are only 
    editorial changes which do not impact the plant design or operations, 
    they cannot increase the probability or the consequences of any 
    accident previously evaluated.
        (2) The proposed changes are editorial only and do not affect the 
    plant design or operation. No new failure modes are introduced by such 
    changes and, therefore, the request will not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        (3) The proposed changes merely correct an editorial oversight. 
    These changes do not alter or delete any technical requirements and, 
    therefore, do not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
        Attorney for licensee: Sheldon Zabel, Esq., Schiff, Hardin and 
    Waite, 7200 Sears Tower, 233 Wacker Drive, Chicago, Illinois 60606.
        NRC Project Director: John N. Hannon.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket No. 
    50-461, Clinton Power Station, Unit No. 1, DeWitt County, Illinois
    
        Date of amendment request: April 18, 1994.
        Description of amendment request: Test methods for carbon adsorber 
    filters specified in Technical Specification Sections 3/4.6.6.3, 
    ``Standby Gas Treatment System,'' and 3/4.7.2, ``Control Room 
    Ventilation System,'' specify the 1979 version of ASTM D3803. The 
    proposed change would delete the year of the standard so that more 
    recent versions of the standard could be used.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        (1) The proposed changes to the Technical Specification 
    surveillance requirements for determining the methyl iodide penetration 
    of carbon samples would not involve a significant increase in the 
    probability or the consequences of any accident previously evaluated 
    because the proposed change merely allows Illinois Power (IP) to 
    utilize a more up-to-date version of the same test method currently 
    specified. More recent versions of the test method are more effective 
    at detecting unsatisfactory charcoal performance because they include 
    equilibration periods to ensure that all samples have a common starting 
    point before being challenged with radioactive gas. The proposed change 
    would not affect the quality of the charcoal or the reliability of the 
    filter subsystems as it only relates to testing and involves no changes 
    to the design or operation of the ventilation subsystems themselves. 
    The updated standards provide more accurate and repeatable test results 
    and do not change the properties or acceptance criteria for these 
    properties. As a result, the performance capabilities of the associated 
    filter subsystems would not be adversely impacted by the proposed 
    change.
        (2) The proposed change would not involve a change in the design or 
    operation of any plant system or component. In addition, the proposed 
    change would not reduce the level of filter train subsystem reliability 
    nor would it create an initiating event for any accident. Because the 
    performance, function, and redundancy of the original design remain 
    unchanged, the proposed change would not create the potential for a new 
    event. Furthermore, since no new types of equipment would be introduced 
    into the plant design and the proposed change would not adversely 
    impact existing equipment, no potential for a different type of 
    malfunction is created by the proposed change. Therefore, this proposed 
    change cannot create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) The margin of safety for the charcoal filter subsystems as 
    defined in the Bases to the Technical Specifications associated with 
    the proposed change refers to the ability of the filters to remove 
    radioiodines. The proposed change would allow IP to upgrade the 
    currently specified test for determining charcoal adsorber performance 
    with one which utilizes the same type of methodology, but provides 
    greater accuracy and repeatability. The newer versions of the test 
    method are more effective at detecting unsatisfactory charcoal 
    performance because they include equilibration periods to ensure that 
    all samples have a common starting point before being challenged with 
    radioactive gas. Thus, the proposed change would not involve a 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
        Attorney for licensee: Sheldon Zabel, Esq., Schiff, Hardin and 
    Waite, 7200 Sears Tower, 233 Wacker Drive, Chicago, Illinois 60606.
        NRC Project Director: John N. Hannon.
    
    Northern States Power Company, Docket No. 50-263, Monticello Nuclear 
    Generating Plant, Wright County, Minnesota
    
        Date of amendment request: March 28, 1994.
        Description of amendment request: The proposed amendment would 
    revise technical specifications Tables 3.2.4 and 4.2.1, to change one 
    of the initiating parameters of the reactor building ventilation 
    isolation system and standby gas treatment system (SGTS) from Low 
    Reactor Water Level to Low Low Reactor Water Level. This revision is 
    being made in order to improve plant performance by reducing the 
    potential for unnecessary secondary containment isolation and SGTS 
    initiations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed amendment will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The function of the Standby Gas Treatment System and secondary 
    containment is to mitigate the consequences of a loss of coolant 
    accident and fuel handling accidents. The proposed changes maintain 
    this capability. The revised Standby Gas Treatment System initiation 
    and secondary containment isolation parameter of low low reactor water 
    level provides the required detection of loss of coolant accidents and 
    is consistent [with] ECCS actuation to mitigate the consequences of 
    this accident. The low low reactor water level instrumentation is set 
    to trip when reactor water level is 6'6'' above the top of the active 
    fuel. This trip currently initiates closure of the Group 1 Primary 
    containment isolation valves, activates the Emergency Core Cooling 
    systems and starts the emergency diesel generator. This trip setting 
    level was chosen to be low enough to prevent spurious operation but 
    high enough to initiate Emergency Core Cooling system operation and 
    primary system isolation so that no melting of the fuel cladding will 
    occur, post accident cooling can be accomplished, and the guidelines of 
    the 10 CFR 100 will not be violated. Therefore, this amendment will not 
    cause a significant increase in the probability or consequences of an 
    accident previously evaluated for the Monticello plant.
        The proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously analyzed. The 
    proposed changes to Technical Specifications for the standby gas 
    treatment system and secondary containment do not alter the function 8 
    of the systems or its interrelationships with other systems. An adverse 
    interaction which could be postulated to occur is the initiation of the 
    Standby Gas Treatment System without a coordinated trip of the 
    Mechanical Vacuum Pump. The Mechanical Vacuum Pump is operated during 
    plant startups to draw a vacuum on the main condenser prior to 
    admission of steam. The Mechanical vacuum discharges to the offgas 
    stack and thus can create a back pressure on the Standby Gas Treatment 
    System, reducing initiation of Standby Gas Treatment System flow below 
    required values. The proposed initiation of Standby Gas Treatment 
    System on low low reactor water level maintains the necessary 
    coordination by having the Standby Gas Treatment System initiate 
    subsequent to isolation or tripping of the Mechanical Vacuum Pump on a 
    low reactor water level signal from the primary containment isolation 
    logic. Therefore, this amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The proposed amendment will not involve a significant reduction in 
    the margin of safety.
        The proposed amendment changes the initiation of the Standby Gas 
    Treatment System and secondary containment isolation from being 
    concurrent with the low reactor water signal (which is indicative that 
    the reactor core is in danger of being inadequately cooled) to being 
    concurrent with reactor low low water level (which is also an indicator 
    that the capability to cool the core is threatened and assures that no 
    melting of the fuel cladding will occur, post accident cooling can be 
    accomplished, and the guidelines of 10 CFR 100 will not be violated). A 
    review of the accident analyses provided in Section 14 of the USAR has 
    determined that these analyses did not specifically credit initiation 
    of the Standby Gas Treatment Systems and secondary containment 
    isolation at the accident precursor reactor water level of low level. 
    Furthermore, this review determined that the low low reactor water 
    level setpoint has no adverse impact on the ability of the Standby Gas 
    treatment System and secondary containment to perform its design basis 
    function as credited in the accident analyses.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Ledyard B. Marsh.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of amendment request: March 24, 1994.
        Description of amendment request: The proposed modification to 
    Technical Specification (TS) Sections 3.11.1.4, 6.9.1.8, and 6.14.1 
    would change the frequency for submitting the Semiannual Radioactive 
    Effluent Release Report to the NRC from semiannually to annually.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed TS changes are administrative in nature. The proposed 
    changes simply involve revising the frequency for submitting the 
    Semiannual Radioactive Effluent Release Report to the NRC from 
    semiannually to annually in order to implement the amended reporting 
    requirements of 10 CFR 50.36a as promulgated in Final Rule 57 FR 39353. 
    Since the information contained in this report is reviewed and 
    evaluated after the effluents are released, no accidents previously 
    evaluated are impacted by the proposed TS changes. Radiological 
    effluent releases from the station will continue to be controlled as 
    required by the TS, including those requirements specified in the 
    Offsite Dose Calculation Manual (ODCM) and Process Control Program 
    (PCP). The proposed TS changes do not involve any changes to the 
    operation or physical configuration of any plant systems or equipment. 
    The proposed changes do not impact any initial or final accident 
    conditions or assumptions previously evaluated. The radiological 
    consequences of these previously evaluated accidents are not affected 
    by the proposed changes.
        Therefore, the proposed TS changes do not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed TS changes are administrative in nature. The proposed 
    changes simply involve revising the frequency for submitting the 
    Semiannual Radioactive Effluent Release Report to the NRC from 
    semiannually to annually in order to implement the amended reporting 
    requirements of 10 CFR 50.36a as promulgated in Final Rule 57 FR 39353. 
    Radiological effluent releases from the station will continue to be 
    controlled as required by the TS, including those requirements 
    specified in the ODCM and PCP. The proposed TS changes do not involve 
    any modifications to plant systems or equipment.
        Therefore, the proposed TS changes do not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        3. The proposed TS changes do not involve a significant reduction 
    in a margin of safety.
        The proposed TS changes are administrative in nature, and will only 
    involve revising the frequency for submitting the Semiannual 
    Radioactive Effluent Release Report to the NRC from semiannually to 
    annually as currently stipulated in 10 CFR 50.36a. The specific 
    radiological effluent release information contained in this report will 
    continue to be provided as required. The station radiological effluent 
    releases will continue to be controlled as required by TS, including 
    those requirements specified in the ODCM and PCP.
        Therefore, the proposed TS changes do not involve a reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J.W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: Charles L. Miller.
    
    South Carolina Electric & Gas Company, South Carolina Public Service 
    Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit 
    No. 1, Fairfield County, South Carolina
    
        Date of amendment request: February 25, 1994.
        Description of amendment request: The proposed Technical 
    Specification (TS) changes would permit the submittal of the 
    Radioactive Effluents Release Report on an annual rather than a 
    semiannual basis; allow changes to the Offsite Dose Calculation Manual 
    (ODCM) to be submitted in the Radioactive Effluent Release Report 
    rather than in the monthly operating report; remove the title of 
    Executive Vice President--Operations from the TS; remove the list of 
    audit frequencies from the TS and place them under Quality Systems 
    management; change the title of Associate Manager, Health Physics to 
    Radiation Protection Manager; remove references to specific letters; 
    remove TS 6.4 on training; and correct various typographical errors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously evaluated 
    because the administrative change does not affect plant operations in 
    any manner.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident than previously evaluated because the 
    proposed change is administrative in nature and no physical alterations 
    of plant configuration or changes to setpoints or operating parameters 
    are proposed.
        3. The proposed license amendment does not involve a significant 
    reduction in a margin of safety. The change is only administrative.
        The NRC staff has reviewed the licensee's analysis and based on 
    this review it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Fairfield County Library, 
    Garden and Washington Streets, Winnsboro, South Carolina 29180.
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218.
        NRC Project Director: William H. Bateman.
    
    South Carolina Electric & Gas Company, South Carolina Public Service 
    Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit 
    No. 1, Fairfield County, South Carolina
    
        Date of amendment request: March 11, 1994.
        Description of amendment request: The proposed Technical 
    Specification (TS) changes would delete surveillance requirement 
    4.8.1.4.a.3, which requires periodic testing of penetration protection 
    fuses, and its associated Basis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
        Fuses are simple protection devices and can only degrade by being 
    more resistive which is in the conservative direction. The proper type 
    and size fuse is assured as part of design, procurement, and initial 
    installation. The testing provides no additional assurance of 
    operability. Therefore, the deletion of periodic retesting of these 
    fuses will not increase the probability or consequences of an accident 
    previously evaluated.
        2. [The proposed amendment will not] [c]reate the possibility of a 
    new or different kind of accident from any previously analyzed.
        The design of the penetration protection and the installation of 
    the fuses has not changed in any way. Any undetected failure of a fuse 
    would fall under single failure criteria. A current limiting fuse must 
    have high electrical current in order to perform its intended function. 
    Any fuse which has opened the circuit through the penetration would be 
    detected. (This is not a concern of the Technical Specifications.) 
    Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety. Deletion 
    of this surveillance requirement will not minimize the intent of this 
    Technical Specification. This TS is to assure continued operability of 
    the containment penetration conductor overcurrent protection which 
    helps to ensure containment integrity. Testing, however, may introduce 
    the potential for damage to the fuses and fuse clips. Therefore, the 
    deletion of this TS requirement will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and based on 
    this review it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Fairfield County Library, 
    Garden and Washington Streets, Winnsboro, South Carolina 29180.
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218.
        NRC Project Director: William H. Bateman.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: November 22, 1993.
        Description of amendment request: The proposed amendment would 
    result in the replacement of most of the analog Riley temperature 
    instrumentation associated with leak detection with digital equipment 
    from the General Electric Company NUMAC product line. Technical 
    Specification changes would be made to instrumentation surveillance 
    requirements for temperature instruments associated with main steam 
    line isolation, reactor water cleanup system isolation, reactor core 
    isolation cooling system isolation, and residual heat removal system 
    isolation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The Technical specifications are proposed to be revised to perform 
    a Channel Functional Test on a semiannual frequency versus the current 
    monthly frequency for both ambient and differential temperature and for 
    the MSL tunnel temperature timer functions, for the above listed piping 
    lines. Additionally, this evaluation addressees the potential for, and 
    implications of, common mode failures due to software, hardware and/or 
    electromagnetic and radio-frequency interference (EMI/RFI).
        The NUMAC instrumentation has certain design features which 
    contribute to its reliability. The replacement NUMAC LDMs are digital 
    instruments that use a microcomputer to monitor the ambient and 
    differential temperatures (also the MSL tunnel temperature timer) and 
    provide outputs and automatic self-testing and calibration. A 
    description of the major design features include: a) isolation of the 
    essential microcomputer by a serial data link from the front panel 
    display (and display microcomputer), b) a self-test system feature that 
    provides automatic testing of internal circuits and reports failures, 
    c) thermocouple failure detection, d) provisions to test the output 
    relays without the use of jumpers (reducing the threat of spurious 
    isolation), and e) two independent built-in instrument power supplies 
    (that automatically switchover to the other supply in the event of 
    failure). Also, several features have been included, among these, a) a 
    hardware ``watchdog'' timer to monitor against software cycling in 
    continuous loops, and b) software structured with the safety-related 
    essential tasks running at the highest priority in the system. These 
    capabilities increase the reliability of the collected data, reduce the 
    possibility of inadvertent isolation and plant shutdowns, reduce the 
    need for frequent calibrations, and reduce the likelihood of common 
    mode failures.
        The NUMAC Leak Detection Monitors will maintain the same 
    environmental and electrical physical independence criteria 
    (qualifications) as the existing Leak Detection System components. The 
    LDMs, the associated thermocouple input units (TCIUs), and relay output 
    units (ROUs) will be mounted seismically such that qualification of 
    these components and the Control Room panels will be maintained. The 
    LDMs are qualified for the PNPP Control Room environment. The LDMs (one 
    per division) will be physically and electrically independent of each 
    other and do not share power supplies, thermocouple inputs, output 
    relays, microcomputer logic units, display units or enclosures and 
    mounting locations. A postulated gross failure of any one NUMAC LDM, 
    such as gross malfunction of the input unit, microcomputer logic unit 
    or the relay output unit, will not propagate to the other NUMAC LDM, 
    such as gross malfunction of the input unit, microcomputer logic unit 
    or the relay output unit, will not propagate to the other NUMAC LDM. 
    Thus, a failure within one NUMAC LDM will not prevent or disable the 
    function of the other NUMAC LDM. A failure within one NUMAC LDM may 
    cause the loss of one division of the isolation trip logic. However, 
    since the other redundant division (the MSLs have three other 
    divisions) will not be affected by this failure, the Leak Detection 
    System will still be able to perform its designed safety-related 
    function and provide the necessary system isolation. This is the same 
    as the current Leak Detection System design basis.
        The possibility of a common mode failure of both NUMAC LDM 
    divisions is minimized by the design of the NUMAC hardware and 
    software, the verification and validation (V&V) of the software to 
    reduce the likelihood of errors, the testing of the software (to 
    discover and eliminate errors), and the design of and testing of the 
    hardware to demonstrate its resistance to EMI/RFI. The NUMAC instrument 
    design features, by effectively eliminating the potential for common 
    mode failures, maintain the Leak Detection System within its current 
    licensing basis. (A discussion of common mode failure protection is 
    presented in more detail in the answer to question two.) Therefore, the 
    design, isolation and separation criteria remain the same.
        Additionally, as described within Chapter 7 of the Updated Safety 
    Analysis Report (USAR), diversity is provided to the ambient and 
    differential temperature monitoring trip functions for the various 
    systems by alternative leak detection methods (such as measuring steam 
    line flow or pressure) that provide backup in the event of the loss of 
    both divisions of the NUMAC Leak Detection Monitors. These alternative 
    leak detection methods are physically separate from those being 
    performed by the NUMAC LDM and constitute a diverse, redundant, safety 
    related backup capable of responding to a design basis line break for 
    the various systems. Therefore, a common mode failure of both LDM 
    divisions would not prevent any of the necessary system isolation from 
    occurring.
        No changes are being made to the isolation logic of the Leak 
    Detection System. No accident initiators or precursors are affected by 
    the proposed changes to the Channel Functional Test surveillance 
    intervals for the various trip functions. One purpose of a Channel 
    Functional Test is to check the instrument setpoints. The NUMAC 
    instrument setpoints are set digitally and do not drift. An engineering 
    evaluation has established that the Channel Functional Test 
    surveillance interval can be extended from one to six months. The 
    potential for common mode failures has been accounted for in the design 
    and measures have been taken to lower the probability of this to an 
    acceptable level (see the answer to question two). Also, alternative 
    leak detection methods exist for this eventuality. Since the NUMAC Leak 
    Detection Monitoring equipment meets or exceeds the design and 
    licensing criteria specified for the Leak Detection System, the 
    proposed upgrade cannot increase the probability of occurrence of any 
    accident previously evaluated.
        A portion of the Leak Detection System logic causes a closure of 
    the Main Steam Isolation Valves on a steam leak signal. This transient, 
    described in Chapter 15 of the USAR, may also occur due to a LDS 
    equipment malfunction. Since this modification replaces some of the 
    existing Riley temperature monitoring instrumentation with more 
    reliable instrumentation the probability of this transient is reduced 
    (no radiological consequences are associated with this event). The LDS 
    is also used to mitigate the consequences of a pipe break outside 
    primary containment by isolating the affected system connected to the 
    Reactor Coolant Pressure Boundary (RCPB). The replacement of the Riley 
    instrumentation with NUMAC LDMs will not change, degrade, or prevent 
    the Leak Detection System response to mitigate the radiological 
    consequences of an accident. Therefore, replacement of the Riley 
    temperature modules with NUMAC Leak Detection Monitors will not 
    significantly increase the consequences of any accident previously 
    evaluated.
        2. The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The single failure criterion requires that any single failure 
    within a safety-related system not prevent proper protective action of 
    the overall system when the system is required to function. The Leak 
    Detection System design is such that a failure of one division will not 
    prevent the system from performing its safety function. Common mode 
    failure protection provisions have been addressed in the NUMAC LDM 
    design.
        The comprehensive General Electric software V&V and configuration 
    management control programs minimize, although they cannot entirely 
    eliminate, the likelihood of a common mode NUMAC instrument failure due 
    to software problems. The hardware (firmware) and software for the PNPP 
    NUMAC Leak Detection Monitors will undergo a formal software 
    verification and validation (V&V) process by General Electric, that is 
    to be completed by the end of the year, equivalent to the one reviewed 
    and approved by the NRC for the safety-related Wide Range Neutron 
    Monitor.
        The NUMAC instruments are designed to minimize both their 
    susceptibility to, and generation of, electromagnetic and radio-
    frequency interference (EMI/RFI) to prevent spurious operations and 
    allow their use in safety-related systems. As part of a broader plan by 
    GE to improve the testing has been performed by GE on the Leak 
    Detection Monitor configuration in order to both expand the overall 
    qualification region, and to obtain test data specific to this 
    application. This testing ensures the qualification of the Thermocouple 
    Input Unit (TCIU), a NUMAC circuit board which is unique to the LDM 
    application, and also extends the NUMAC EMI/RFI qualification region to 
    include both higher and lower frequencies than previously tested.
        The NUMAC instrument design concept has undergone review by the 
    NRC, and the initial instruments of the NUMAC product line (the 
    Logarithmic Radiation Monitor and Wide Range Neutron Monitoring System) 
    have received NRC approval via Safety Evaluation of the associated GE 
    Licensing Topical Reports. The various types of NUMAC equipment in 
    operation at other nuclear power plants have components and software 
    modules which are similar to and in some instance identical to the 
    NUMAC LDMs. Therefore, based on the NRC reviewed and approved NUMAC 
    software and hardware control programs instituted by GE, the design 
    features to minimize software/hardware (or their interface) problems, 
    design features to minimize susceptibility to EMI/RFI, and testing to 
    demonstrate resistance to EMI/RFI, installation of NUMAC Leak Detection 
    Monitors at the PNPP does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The proposed changes do not involve a significant reduction in a 
    margin of safety.
        The replacement of the analog Riley temperature modules with the 
    microcomputer based NUMAC Leak Detection Monitors will not affect any 
    design conditions or impact the margins of safety for the various Leak 
    Detection System monitored parameters in the Technical Specification 
    Table 3.3.2-2 will not be changed or affected by this modification. 
    Only the CHANNEL FUNCTIONAL test interval is being extended.
        The NUMAC Leak Detection Monitor design, with the attention paid 
    towards minimizing the potential for, and the effect of, software/
    hardware and/or EMI/RFI related problem or common mode failures and 
    resulting operational experience has demonstrated that replacement of 
    the existing Riley temperature modules with NUMAC Leak Detection 
    Monitors would not result in a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: February 8, 1994, as supplemented March 
    25, 1994.
        Description of amendment request: The amendment would revise the 
    WNP-2 Technical Specifications. Specifically, the amendment would 
    increase the stroke time, as specified in Table 3.6.3-1, for reactor 
    core isolation cooling (RCIC) valve RCIC-V-8, from 13 seconds to 26 
    seconds and the note (j) reference would be deleted from RCIC-V-8 and 
    RCIC-V-63. The note (j) indicates that the stroke time specified in the 
    Table reflects the requirement for containment isolation only.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. This proposed action does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    RCIC-V-8 and V-63 are containment isolation valves and are normally 
    open. Failure of the valves to open or close cannot cause an accident. 
    The mitigating capability of RCIC-V-8 and V-63 is not changed in that 
    the valves will continue to be closed within the established time 
    limits. This ensures protection of the safety related equipment 
    necessary for continued compliance with the requirements of General 
    Design Criterion 4. In those accidents which involve a source term and 
    potential adverse dose release consequences, no credit is taken for the 
    closing of the valves; therefore the increase in the allowable time for 
    closing does not increase the consequences of those accidents.
        2. This proposed action does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. The 
    requested Technical Specifications change does not represent a change 
    in modes of operation. It does not, in itself, require physical 
    modification to the plant, although it will be used to allow a gear 
    change in RCIC-MO-8. The new gears represent a standard configuration 
    for Limitorque motor operators and will require a routine design 
    change. The required Technical Specification change maintains the 
    licensing basis for the plant as discussed in response to question 1. 
    Hence, no new or different kind of accident is possible as a result of 
    implementing this change.
        3. This proposed action does not involve a significant reduction in 
    a margin of safety. The increase in stroke time will increase the peak 
    temperature in the HELB profiles and thereby decrease the margin 
    available from the equipment qualification limits. However, sufficient 
    margin remains to assure the equipment operability is maintained and 
    there is no reduction in the margin of safety. Additionally, there is 
    no reduction in the margin of safety because increasing the stroke time 
    will not change the postulated radiological releases.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
        Attorney for licensee: M.H. Philips, Jr., Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502.
        NRC Project Director: Theodore R. Quay.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of amendments request: April 14, 1994.
        Description of amendments request: The proposed change would 
    relocate the instrument response time tables 3.3.1-2, Reactor 
    Protection System (RPS) Response Times; 3.3.2-3, Isolation System 
    Instrumentation (ISI) Response Time; and 3.3.3-3, Emergency Core 
    Cooling System (ECCS) Response Times, from the Technical Specifications 
    to the Updated Final Safety Analysis Report. The RPS, ISI, and ECCS 
    instrument limiting conditions for operation (LCO) will be revised to 
    read that the instruments ``shall be operable'' without a reference to 
    a specific response time table in these LCOs. The references to the 
    response time tables will also be deleted from the Surveillance 
    Requirements.
        Date of publication of individual notice in Federal Register: April 
    26, 1994 (59 FR 21785).
        Expiration date of individual notice: May 26, 1994.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana
    
        Date of application for amendment: January 14, 1994.
        Brief description of amendment request: The proposed amendment 
    would revise various instrumentation technical specifications by 
    extending the allowable outage times (AOTs) of the instruments, and by 
    increasing their channel functional surveillance test intervals (STIs) 
    to quarterly. The amendment also revises certain technical 
    specification actions to address loss-of-function concerns associated 
    with the AOT and STI changes.
        Date of individual notice in Federal Register: April 26, 1994(59 FR 
    21787).
        Expiration date of individual notice: May 26, 1994.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana
    
        Date of application for amendment: February 22, 1994.
        Brief description of amendment request: The proposed amendment 
    would revise the technical specifications (TS) for the main steam-
    positive leakage control system (MS-PLCS) and the penetration valve 
    leakage control system (PVLCS) to be consistent with the requirements 
    contained in NUREG-1434, ``Standard Technical Specifications, General 
    Electric Plants (BWR/6).''
        Date of individual notice in Federal Register: March 10, 1994 (59 
    FR 11331).
        Expiration date of individual notice: April 11, 1994.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana
    
        Date of application for amendment: March 3, 1994.
        Brief description of amendment request: The amendment would revise 
    the technical specifications in accordance with the guidance provided 
    by Generic Letter 93-08, ``Relocation of Technical Specification Tables 
    of Instrument Response Time Limits.'' Generic Letter 93-08 recommends 
    the removal and subsequent relocation of various technical 
    specification tables which denote instrument and system response time 
    limits.
        Date of individual notice in Federal Register: March 16, 1994 (59 
    FR 12380).
        Expiration date of individual notice: April 15, 1994.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units 1, 2, 
    and 3, Maricopa County, Arizona
    
        Date of application for amendments: October 26, 1993, as 
    supplemented March 28, 1994.
        Brief description of amendments: The licensee is requesting a 
    revision to TS 5.3.1 for Palo Verde Nuclear Generating Station Units 1, 
    2, and 3 that will increase the maximum allowable fuel enrichment from 
    4.05 weight percent U-235 to 4.30 weight percent U-235. There was no 
    change requested to the current 52,000 MWD/MTU burnup. The licensee 
    provided a supplemental letter dated March 28, 1994, at the request of 
    the NRC to bring TS 5.3.1 into conformance with Generic Letter 90-02, 
    Supplement 1 and to clarify assumptions used in the Fuel Handling 
    Accident Analysis.
        Date of issuance: April 19, 1994.
        Effective date: April 19, 1994, to be implemented within 45 days of 
    issuance.
        Amendment Nos.: 74, 60 and 46.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: January 19, 1994 (59 FR 
    2860) The additional information contained in the supplemental letter 
    dated March 28, 1994, was clarifying in nature and thus within the 
    scope of the initial notice and did not affect the NRC staff's proposed 
    no significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated April 19, 1994. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of application for amendments: September 1, 1992.
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) 3/4.4.3, ``Relief Valves,'' to improve the 
    reliability of the reactor coolant system's power-operated relief 
    valves (PORVs) and their associated block valves for overpressure 
    protection during normal operation and anticipated transients. The 
    amendments also revise TS 3/4.4.9, ``Pressure/Temperature Limits,'' to 
    improve the availability of the PORVs for low temperature overpressure 
    protection. Accompanying changes are also made to the associated TS 
    Bases. These revisions were made in response to Generic Letter 90-06, 
    ``Resolution of Generic Issue 70, `Power-Operated Relief Valve and 
    Block Valve Reliability,' and Generic Issue 94, `Additional Low-
    Temperature Overpressure Protection for Light-Water Reactors,' pursuant 
    to 10 CFR 50.54 (f).''
        Date of issuance: April 20, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 188 and 165.
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 30, 1992 (57 
    FR 45076).
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated April 20, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: February 4, 1994.
        Brief description of amendment: The amendment revises TS 
    Surveillance Requirement 4.6.4.1 to delete the 12-hour channel check, 
    thereby eliminating the need for continuous operation of the hydrogen 
    monitors.
        Date of issuance: April 26, 1994.
        Effective date: April 26, 1994.
        Amendment No. 47.
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10001) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. STN 
    50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: March 21, 1994, as supplemented 
    March 24, 1994.
        Brief description of amendments: The amendments add a one-time 
    revision to Technical Specification (TS) 3/4.7.1.1 to permit continued 
    activities at all four units with main steam Code safety valve lift 
    setpoint tolerances of 3%. The duration of this amendment 
    is until May 9, 1994, at which time the tolerances will be reset to 
    1%. A statement has also been added to TS 4.7.1.1 for 
    Braidwood stating that the provisions of TS 4.0.4 are not applicable to 
    Braidwood, Unit 1, Cycle 5 until initial entry into Mode 2 from its 
    refueling outage.
        Date of issuance: April 18, 1994.
        Effective date: April 18, 1994.
        Amendment Nos.: 61, 61, 49, and 49.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    Amendment revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes (59 FR 14685 dated March 29, 1994). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination within 15 days. No 
    comments have been received. The notice also provided an opportunity to 
    request a hearing by April 29, 1994, but indicated that if the 
    Commission makes a final no significant hazards consideration 
    determination any such hearing would take place after issuance of the 
    amendment. The Commission's related evaluation of the amendment and 
    final no significant hazards consideration determination is contained 
    in a Safety Evaluation dated April 18, 1994.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: September 29, 1993, as 
    supplemented by letter dated April 8, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specification Section 3.9.A.5 and Tables 3.9-1 and 4.10-2 to delete 
    controls for the 21, 22, and 23 Boron Monitor Tanks, which are no 
    longer in service.
        Date of issuance: April 28, 1994.
        Effective date: As of the date of issuance to be implemented after 
    the inlet and outlet lines of the 21, 22, and 23 Boron Monitor Tanks 
    have been cut and capped.
        Amendment No.: 169.
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1993 (58 
    FR 62154)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of application for amendment: May 23, 1993.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.4.3.2.d and related Table 3.4.3.2-1 by changing 
    the allowable leakage for certain low pressure coolant injection (LPCI) 
    line pressure isolation valves and revises Table 3.6.3-1 to remove the 
    designation as containment isolation valves from the LPCI injection 
    reverse flow check and bypass valves. The related Bases are also 
    changed. Concurrently, the Commission granted an exemption from the 
    requirements of 10 CFR Part 50, Appendix J, III.C. for performing Type 
    C containment integrated leak rate tests of the containment isolation 
    valves in the low pressure coolant injection lines of the residual heat 
    removal system and to perform alternative testing.
        Date of issuance: April 22, 1994.
        Effective date: April 22, 1994, with full implementation within 45 
    days.
        Amendment No.: 98.
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: September 1, 1993 (58 
    FR 46227) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 22, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: February 24, 1993.
        Brief description of amendment: The amendment corrected 
    typographical errors in the plant technical specifications (TSs). These 
    errors were introduced in the original ANO-1 TS, and in subsequent 
    amendments. These changes are administrative in nature and are intended 
    to improve the readability of the plant technical specifications 
    without changing the meaning or intent of any specifications.
        Date of issuance: April 26, 1994.
        Effective date: April 26, 1994.
        Amendment No.: 171.
        Facility Operating License No. DPR-51. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67843)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: November 16, 1993, as supplemented by 
    letter dated April 5, 1994.
        Brief description of amendment: The amendment revised the Technical 
    Specifications to provide acceptable conditions for operation when the 
    core operating limit supervisory system (COLSS) is out of service and 
    either or both control element assembly calculators (CEACs) are 
    operable.
        Date of issuance: April 22, 1994.
        Effective date: April 22, 1994.
        Amendment No.: 93.
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    620) The additional information contained in the supplemental letter 
    dated April 5, 1994, withdrew a portion of the original application and 
    thus, was within the scope of the initial notice and did not affect the 
    staff's proposed no significant hazards consideration determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated April 22, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: February 14, 1994.
        Brief description of amendment: The amendment revised the Technical 
    Specifications in response to Generic Letter 93-08 issued by the NRC 
    and dated December 29, 1993, by relocating the reactor trip system and 
    engineered safety features actuation system response time limits to the 
    updated final safety analysis report.
        Date of issuance: April 22, 1994.
        Effective date: April 22, 1994.
        Amendment No.: 94.
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12360) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 22, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: February 25, 1992.
        Brief description of amendments: The amendments relate to your 
    application dated February 25, 1992, which requested a 40-year 
    operating license commencing from the date of issuance of the operating 
    license and, accordingly, would extend the operating license expiration 
    date for Turkey Point Units 3 and 4 to July 19, 2012 and April 10, 
    2013, respectively.
        Date of issuance: April 20, 1994.
        Effective date: April 20, 1994.
        Amendment Nos. 162 and 156.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 15, 1992 (57 FR 
    13130) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 20, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: December 28, 1993.
        Brief description of amendments: These amendments include steam 
    generator overfill protection in the Technical Specifications in 
    response to Generic Letter 89-19, Request for Action Related to 
    Resolution of Unresolved Safety Issue A-47 ``Safety Implications of 
    Control Systems in LWR Nuclear Power Plants.''
        Date of issuance: April 28, 1994.
        Effective date: April 28, 1994.
        Amendment Nos. 163 and 157.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10007) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 28, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: March 14, 1994.
        Brief description of amendment: The amendment changes the Millstone 
    Unit 2 Technical Specifications (TS) to provide a one-time extension of 
    the surveillance frequency from the required 18-month to the next 
    refueling outage but no later than September 30, 1994, of the power 
    operated valves in the service water system (TS 4.7.4.1.b) and in the 
    boron injection flowpath (TS 4.1.2.2.c). This extends the surveillance 
    for these valves approximately 5 months.
        Date of issuance: April 22, 1994.
        Effective date: April 22, 1994.
        Amendment No.: 173.
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 23, 1994 (59 FR 
    13751). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 22, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    Northeast Nuclear Energy Company, Docket Nos. 50-245, 50-336, and 50-
    423, Millstone Nuclear Power Station, Units 1, 2 and 3, New London 
    County, Connecticut
    
        Date of application for amendment: December 22, 1993.
        Brief description of amendment: The amendments revise the Technical 
    Specifications (TS) as follows:
        1. Change the title of the Nuclear Station Director to Senior Vice 
    President--Millstone Station.
        2. Remove the requirement to provide a copy of Plant Operations 
    Review Committee (PORC) and Site Operations Review Committee (SORC) 
    meeting minutes to the Executive Vice President--Nuclear. The Senior 
    Vice President--Millstone Station replaces the Executive Vice 
    President--Nuclear for receipt of PORC and SORC meeting minutes.
        3. Make editorial changes to the Millstone Unit No. 1 TS Index.
        4. Correct a typographical error in Section 6.2.1.d of the 
    Millstone Unit No. 1 TS.
        5. Correct a typographical error in Section 6.5.3.1.a of the 
    Millstone Unit No. 3 TS.
        Date of issuance: April 26, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 74, 174, and 90.
        Facility Operating License No. DPR-21, DPR-65, AND NPF-49. 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7693) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: April 19, 1993, as supplemented 
    by letter dated April 18, 1994.
        Brief description of amendments: These amendments extend 
    surveillance test interval and allowed outage times for the containment 
    isolation actuation instrumentation.
        Date of issuance: April 26, 1994.
        Effective date: April 26, 1994.
        Amendment Nos. 69 and 32.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34086) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: May 6, 1993, as supplemented by 
    letter dated April 18, 1994.
        Brief description of amendments: These amendments extend 
    surveillance test interval and allowed outage times for selected 
    actuation instrumentation and makes editorial changes.
        Date of issuance: April 26, 1994.
        Effective date: April 26, 1994.
        Amendment Nos. 70 and 33.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34087) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Public Service Electric and Gas Company 
    Delmarva Power and Light Company, and Atlantic City Electric Company, 
    Docket Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit 
    Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 19, 1993.
        Brief description of amendments: These amendments eliminate the 
    listing of specific position titles for the Plant Operations Review 
    Committee (PORC) composition in favor of allowing the Plant Manager to 
    appoint PORC members. This revision eliminates the need to change the 
    TS in the future whenever a position title is changed.
        Date of issuance: April 26, 1994.
        Effective date: April 26, 1994.
        Amendments Nos.: 190 and 195.
        Facility Operating License Nos. DPR-44 and DPR-56: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 5, 1994 (59 FR 
    628) The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated April 26, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (Regional Depository) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: January 31, 1994.
        Brief description of amendment: This amendment to the Appendix B 
    Technical Specifications (TSs), the Radiological Effluent TSs, revised 
    Section 3.5, and the associated Bases, to establish a threshold level 
    below which there will be no requirement to perform grab samples and 
    isotopic analyses of steam jet-air ejector (SJAE) effluent and revised 
    TS Table 3.10-1 to change the actions required when entering an SJAE 
    limiting condition for operation. Additionally, the amendment revised 
    the TSs to clarify instructions and make editorial corrections which 
    are administrative in nature.
        Date of issuance: April 25, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 211.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10014).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 25, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: March 12, 1993.
        Brief description of amendment: The amendment revised the Technical 
    Specifications (TS) to incorporate the changes listed below:
        (1) The frequency of high pressure water fire protection system 
    testing (specified in TS Section 4.12.A.1) was changed to accommodate 
    operation on a 24-month cycle.
        (2) The frequency of fire pump diesel engine testing (specified in 
    TS Section 4.12.A.2) was changed to accommodate operation on a 24-month 
    cycle.
        (3) The frequency of electrical tunnel, diesel generator building, 
    and containment fan cooler fire protection spray and/or sprinkler 
    system testing (specified in TS Section 4.12.B.1) was changed to 
    accommodate operation on a 24-month cycle.
        (4) The frequency of fire barrier penetration seal inspection 
    (specified in TS Section 4.12.C.1) was changed to accommodate operation 
    on a 24- month cycle.
        (5) The frequency of fire detection system testing (specified in TS 
    Section 4.12.D.1) was changed to accommodate operation on a 24-month 
    cycle.
        (6) The frequency of fire hose station testing (specified in TS 
    Section 4.12.E.1) was changed to accommodate operation on a 24-month 
    cycle.
        (7) The frequency of CO2 fire protection system testing 
    (specified in TS Section 4.12.G.1) was changed to accommodate operation 
    on a 24-month cycle. A new requirement was also added to exercise the 
    fire dampers on an annual basis.
        These changes followed the guidance provided in Generic Letter 91-
    04, ``Changes in Technical Specification Surveillance Intervals to 
    Accommodate a 24-Month Fuel Cycle,'' as applicable.
        In addition, TS Section 4.12 was reformatted, in its entirety, and 
    several administrative changes were made to improve clarity.
        Date of issuance: April 20, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 146.
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1993 (58 FR 
    25862) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 20, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: March 4, 1994.
        Brief description of amendment: This amendment adds a new TS 3/
    4.10.8, ``Inservice Leak and Hydrostatic Testing,'' to the Hope Creek 
    Generating Station TSs. The amendment also includes corresponding 
    changes to the TS Index, Table 1.2, ``OPERATIONAL CONDITIONS,'' and 
    provides Bases for TS 3/4.10.8. The added TS 3/4.10.8 permits the unit 
    to remain in OPERATIONAL CONDITION 4 with the average reactor coolant 
    temperature being increased above 200 deg.F, but not to exceed 
    212 deg.F, and certain OPERATIONAL CONDITION 3 Limiting Conditions for 
    Operation for secondary containment isolation, secondary containment 
    integrity and filtration, recirculation and ventilation system (FRVS) 
    operability being met.
        Date of issuance: April 18, 1994.
        Effective date: April 18, 1994.
        Amendment No.: 69.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12384).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 18, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: December 23, 1992, as 
    supplemented August 12, 1993 and January 21, 1994 (TS 328).
        Brief description of amendments: The amendments modify the 
    operability requirements for the low pressure coolant injection (LPCI) 
    mode of the residual heat removal (RHR) system while the reactor is 
    shut down. The amendments permit the RHR system to be considered 
    operable for LPCI when aligned for shutdown cooling if it can be 
    manually realigned and is not otherwise inoperable.
        Date of issuance: April 19, 1994.
        Effective date: April 19, 1994.
        Amendment Nos.: 204, 223, and 177.
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68:
        Date of initial notice in Federal Register: March 31, 1993 (58 FR 
    16873).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 19, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: February 7, 1994 (TS 93-11).
        Brief description of amendments: The amendments replace the wording 
    in Surveillance Requirement 4.7.9.i, ``Snubber Service Life Program,'' 
    with that from the Westinghouse Electric Corporation Standard TS, 
    Revision 4a. In addition, the amendments delete the wording in SR 
    4.7.9.c, ``Snubber Visual Inspection Performance and Evaluation,'' that 
    is inconsistent with Generic Letter 90-09.
        Date of issuance: April 18, 1994.
        Effective date: April 18, 1994.
        Amendment Nos.: 179--Unit 1 171--Unit 2.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: February 7, 1994.
        The Commission's related evaluation of the amendments are contained 
    in a Safety Evaluation dated April 18, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: February 7, 1994 (TS 93-19).
        Brief description of amendments: The amendments revise Technical 
    Specification 5.3.1 to allow the substitution of filler rods for fuel 
    rods in fuel assemblies by incorporating the guidance in Generic Letter 
    90-02, Supplement 1.
        Date of issuance: April 18, 1994.
        Effective date: April 18, 1994.
        Amendment Nos.: 180--Unit 1 172--Unit 2.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12367) The Commission's related evaluation of the amendments are 
    contained in a Safety Evaluation dated April 18, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: September 28, 1992.
        Brief description of amendment: The amendment revised Technical 
    Specification (TS) 2.2, Limiting Safety System Settings, TS 3.3.1, 
    Reactor Protection System Instrumentation, and TS 3.3.2, Isolation 
    Actuation Instrumentation by removing the functions associated with the 
    main steam line radiation monitors.
        Date of issuance: April 22, 1994.
        Effective date: April 22, 1994.
        Amendment No. 58.
        Facility Operating License No. NPF-58. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 6, 1993 (58 FR 
    598) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 22, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: July 28, 1992, as supplemented 
    on February 17, 1993.
        Brief description of amendment: The proposed amendment would delete 
    Technical Specification (TS) 3/4.9.9, ``Refueling Operations--
    Containment Purge and Exhaust Isolation System,'' and its bases, 
    because of its redundancy to other TSs that address the operability 
    requirements of the containment purge and exhaust isolation system. 
    Also, the proposed amendment would revise TS 3/4.3.2, ``Safety System 
    Instrumentation--Safety Features Actuation System Instrumentation,'' 
    and TS 3.4.9.4, ``Refueling Operations--Containment Penetrations,'' and 
    its bases. The effect of this proposed change would be to allow the 
    bypass of the safety features actuation system in Mode 6, 
    ``Refueling,'' by the use of the containment purge and exhaust system 
    noble gas monitor in conjunction with manual closure of the containment 
    purge and exhaust isolation valves instead of automatic closure.
        Date of issuance: April 15, 1994.
        Effective date: April 15, 1994.
        Amendment No. 186.
        Facility Operating License No. NPF-3. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 6, 1993 (58 FR 
    599) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 15, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 50-
    339, North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of application for amendments: October 8, 1993.
        Brief description of amendments: The amendments revise the 
    technical specifications (TS) by deleting tables listing certain 
    components from the TS and relocating the lists to plant procedures in 
    accordance with the guidance provided in NRC Generic Letter 91-08, 
    ``Removal of Component Lists from Technical Specifications.''
        Date of issuance: April 22, 1994.
        Effective date: April 22, 1994.
        Amendment Nos.: 181 and 162.
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: October 27, 1993 (58 FR 
    57860) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 22, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: July 29, 1993, as supplemented 
    by letters dated March 11 and 17, 1994.
        Brief description of amendment: The amendment modifies the 
    Technical Specifications (TS) to reflect a new refueling mast. 
    Specifically, the amendment adds new values for protective features in 
    the TS to reflect the new refueling mast. Values for the old refueling 
    mast are retained in the TS.
        Date of issuance: April 29, 1994.
        Effective date: April 29, 1994.
        Amendment No.: 121.
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14900) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 29, 1994.
        Public comments on proposed no significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301 Point 
    Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks Manitowoc 
    County, Wisconsin
    
        Date of application for amendments: February 26, 1993.
        Brief description of amendments: The amendments adding operating 
    conditions and limiting conditions for operation for the atmospheric 
    steam dump valves, the crossover steam dump system, the turbine stop 
    and governor valves, and the various turbine overspeed protection 
    features installed at the Point Beach Nuclear Plant. Additionally, the 
    amendments revised the surveillance requirements for the auxiliary 
    feedwater system, and added explanatory text to the bases for Sections 
    15.3.4 and 15.4.8.
        Date of issuance: April 20, 1994.
        Effective date: April 20, 1994.
        Amendment Nos.: 147 and 151.
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 18, 1993 (58 FR 
    43939) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 20, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: October 21, 1993, as supplemented by 
    letters dated March 14, 1994, and April 18, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specification Sections 6.5.1, Plant Safety Review Committee (PSRC) and 
    6.8, Procedures and Programs, in order to allow implementation of a 
    Qualified Reviewer Program for the review and approval of new 
    procedures and procedure changes. Technical Specification 6.5.1.6, PSRC 
    Responsibilities, has also been revised in accordance with Generic 
    Letter 93-07, ``Modification of Technical Specification Administrative 
    Control Requirements for Emergency and Security Plans,'' to delete 
    requirements for PSRC review of the Emergency Plan and Security Plan 
    and related implementing procedures.
        Date of Issuance: April 28, 1994.
        Effective date: April 28, 1994, to be implemented within 120 days 
    of issuance.
        Amendment No.: Amendment No. 73.
        Facility Operating License No. NPF-42. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1993 (58 
    FR 62159) The March 14, 1994, and April 18, 1994, supplemental letters 
    provided additional clarifying information and revised the 
    implementation period and did not change the initial no significant 
    hazards consideration. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated April 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room Locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
        Dated at Rockville, Maryland, this 4th day of May 1994.
    
        For the Nuclear Regulatory Commission.
    Jack W. Roe,
    Director Division of Reactor Projects--III/IV Office of Nuclear Reactor 
    Regulation.
    [FR Doc. 94-11226 Filed 5-11-94; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
05/12/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-11226
Dates:
April 19, 1994, to be implemented within 45 days of issuance.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: May 12, 1994