99-12494. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 96 (Wednesday, May 19, 1999)]
    [Notices]
    [Pages 27315-27339]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-12494]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
    
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from April 24, 1999, through May 7, 1999. The 
    last biweekly notice was published on May 5, 1999.
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed no Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
    
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
    
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
    
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
    
        By June 18, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
    
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been
    
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    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
    
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
    
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
    
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
    
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
    
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
    
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
    
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: March 3, 1999.
    
        Description of amendment request: The proposed amendment would 
    change the reactor vessel (RV) surveillance capsule pull interval from 
    approximately 15 effective full power (EFPY) years to 18 EFPY in 
    Technical Specification (TS) Table 4.6-3.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below: The operation of Pilgrim in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    Pilgrim plant's physical configuration and operational practices are 
    not changed by this proposed change. The licensee is only proposing to 
    change the TS withdrawal schedule for the RV surveillance capsule. This 
    change does not affect any of the current accident mitigation features 
    of the facility or the sequence of any accidents previously analyzed. 
    For the reasons given above, deferral of withdrawal of Pilgrim's second 
    capsule for at least one additional cycle (or 3 EFPY) does not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
    
        The operation of Pilgrim in accordance with the proposed amendment 
    will not create the possibility of a new or different kind of accident 
    from any accident previously evaluated. As discussed in the above 
    narrative, the deferral of the second capsule pull at Pilgrim does not 
    change any of the design features or operation of the facility but does 
    defer a TS surveillance. Pilgrim's current TS pressure-temperature (P-
    T) curves are conservative and will remain so even if the RV 
    surveillance capsule is not pulled this outage. The data from the first 
    RV capsule supports this conclusion. Because the RV capsule pull 
    schedule is being deferred, the P-T curves, which can be modified based 
    on the data from the RV capsule surveillance, will not be changed. The 
    deferral of the withdrawal of Pilgrim's second RV surveillance capsule 
    does not change the design features or operation of the facility and 
    the existing P-T curves have not changed, therefore, the TS change will 
    not create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
    
        The operation of Pilgrim in accordance with the proposed amendment 
    will not involve a significant reduction in the margin of safety.
    
        The capsule pull is a surveillance technique that provides data for 
    modification of the P-T curves. The methods used to develop the 
    temperatures associated with these curves are regarded as conservative. 
    The data from the first RV capsule supported this conclusion. Because 
    the P-T curves have not changed and have been determined to be 
    conservative, the margins of safety that were previously established 
    have not changed. Therefore, deferral of the withdrawal of Pilgrim's 
    second RV surveillance capsule will not involve a significant reduction 
    in the margin of safety.
    
        Based on this review, it appears that the three standards of 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the
    
    [[Page 27317]]
    
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Plymouth Public Library, 132 
    South Street, Plymouth, Massachusetts 02360.
    
        Attorney for licensee: J. Fulton, Boston Edison Company, 800 
    Boylston Street, 36th Floor, Boston, Massachusetts 02199.
    
        NRC Section Chief: James W. Clifford.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: March 30, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise Section 4.0, Surveillance Requirements, of the Technical 
    Specifications (TSs). Specifically, Section 4.0.2 would be added to 
    allow a 24-hour grace period for performing inadvertently missed 
    surveillance.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
    
        Response: No. This proposed change will result in either the 
    plant condition either remaining unchanged (i.e., the system or 
    component is declared operable) or in the plant proceeding to a 
    shutdown condition (i.e., the system or component is declared 
    operable). If at the end of the 24-hour interval, it is necessary to 
    proceed to shutdown, this shutdown is indistinguishable from any 
    shutdown where a system or component is declared inoperable. 
    Allowing an additional 24 hours to perform the surveillance balances 
    the risks associated with an allowance for completing the 
    surveillance within this 24-hour period against the risks associated 
    with the potential for a plant upset and challenge to safety systems 
    when the alternative is a shutdown to comply with the action 
    requirements before the surveillance can be completed. Therefore, 
    the proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Does the proposed amendment create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated?
        Response: No. This proposed change will result in either the 
    plant condition either remaining unchanged (i.e., the system or 
    component is declared operable) or in the plant proceeding to a 
    shutdown condition (i.e., the system or component is declared 
    operable). If at the end of the 24-hour interval, it is necessary to 
    proceed to shutdown, this shutdown is indistinguishable from any 
    shutdown where a system or component is declared inoperable. 
    Allowing an additional 24 hours to perform the surveillance balances 
    the risks associated with an allowance for completing the 
    surveillance within this 24-hour period against the risks associated 
    with the potential for a plant upset and challenge to safety systems 
    when the alternative is a shutdown to comply with the action 
    requirements before the surveillance can be completed. Therefore, 
    the proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response: No. This proposed change will result in either the 
    plant condition either remaining unchanged (i.e., the system or 
    component is declared operable) or in the plant proceeding to a 
    shutdown condition (i.e., the system or component is declared 
    operable). If at the end of the 24-hour interval, it is necessary to 
    proceed to shutdown, this shutdown is indistinguishable from any 
    shutdown where a system or component is declared inoperable. 
    Allowing an additional 24 hours to perform the surveillance within 
    this 24-hour period against the risks associated with the potential 
    for a plant upset and challenge to safety systems when the 
    alternative is a shutdown to comply with the action requirements 
    before the surveillance can be completed . Therefore, the proposed 
    change does not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
    
        NRC Section Chief: S. Singh Bajwa.
    
    Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: July 22 and October 22, 1998; May 6, 
    1999.
    
        Description of amendment request: The amendments would revise the 
    Technical Specifications (TS) to reflect the licensee's planned use of 
    fuel supplied by Westinghouse. The staff has published a Notice of 
    Consideration of Issuance of Amendments and Proposed No Significant 
    Hazards Consideration Determination on November 18, 1998 (63 FR 64108) 
    covering the July 22 and October 22, 1998, submittals. In the May 6, 
    1999, submittal the licensee proposed to expand the original amendment 
    request, revising Section 5.6.5 of the Technical Specifications. 
    Section 5.6.5 specifies a list of NRC-approved topical reports that the 
    licensee is required to use to determine reactor core operating limits. 
    The licensee proposed to update this list to show the current approval 
    status of these topical reports.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration for the proposed changes conveyed by the May 6, 1999, 
    submittal. The NRC staff has reviewed the licensee's analyses against 
    the standards of 10 CFR 50.92(c). The NRC-staff's analysis is presented 
    below.
    First Standard
    
        No. The proposed changes to Section 5.6.5 will not affect the 
    safety function and will not involve any change to the design or 
    operation of any plant system or component. The topical reports were 
    previously approved by the NRC staff under separate licensing actions. 
    The use of methodologies in these approved topical reports will ensure 
    that previously evaluated accidents remain bounding. Therefore, no 
    accident probabilities or consequences will be impacted.
    Second Standard
    
        No. The proposed changes would not lead to any hardware or 
    operating procedure change. Hence, no new equipment failure modes or 
    accidents from those previously evaluated will be created.
    Third Standard
    
        No. Margin of safety is associated with confidence in the design 
    and operation of the plant; specifically, the ability of the fission 
    product barriers to perform their design functions during and following 
    an accident. The proposed changes to Section 5.6.5 do not involve any 
    change to plant design, operation, or analysis. Thus, the margin of 
    safety previously analyzed and evaluated is maintained.
    
        Based on this analysis, it appears that the three standards of 10 
    CFR 50.92(c) are satisfied for the proposed changes to Section 5.6.5. 
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
    
    
    [[Page 27318]]
    
    
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
        Attorney for licensee: Ms. Lisa F. Vaughn , Legal Department 
    (PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte, 
    North Carolina.
    
        NRC Section Chief: Richard L. Emch, Jr.
    
    Duke Energy Corporation, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: April 5, 1999.
    
        Description of amendment request: The proposed amendments would 
    provide revised spent fuel pool storage configurations, revised spent 
    fuel pool storage criteria, and revised fuel enrichment and burnup 
    requirements which take credit for soluble boron in maintaining 
    acceptable margins of subcriticality in the spent fuel storage pools. 
    Also, the proposed amendments would provide additional criteria for 
    ensuring acceptable levels of subcriticality in the spent fuel storage 
    pools.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will the change involve a significant increase in the 
    probability or consequence of an accident previously evaluated?
        No, based upon the following:
    
    Dropped Fuel Assembly
    
        There is no significant increase in the probability of a fuel 
    assembly drop accident in the spent fuel pools when considering the 
    degradation of the Boraflex panels in the spent fuel pool racks 
    coupled with the presence of soluble boron in the spent fuel pool 
    water for criticality control. The handling of the fuel assemblies 
    in the spent fuel pool has always been performed in borated water, 
    and the quantity of Boraflex remaining in the racks has no affect on 
    the probability of such a drop accident.
        The criticality analysis showed that the consequences of a fuel 
    assembly drop accident in the spent fuel pools are not affected when 
    considering the degradation of the Boraflex in the spent fuel pool 
    racks and the presence of soluble boron.
    
    Fuel Misloading
    
        There is no significant increase in the probability of the 
    accidental misloading of spent fuel assemblies into the spent fuel 
    pool racks when considering the degradation of the Boraflex in the 
    spent fuel pool racks and the presence of soluble boron in the pool 
    water for criticality control. Fuel assembly placement and storage 
    will continue to be controlled pursuant to approved fuel handling 
    procedures to ensure compliance with the Technical Specification 
    requirements. These procedures will be revised as needed to comply 
    with the revised requirements which would be imposed by the proposed 
    Technical Specification changes.
        There is no increase in the consequences of the accidental 
    misloading of spent fuel assemblies into the spent fuel pool racks 
    because criticality analyses demonstrate that the pool will remain 
    subcritical following an accidental misloading if the pool contains 
    an adequate boron concentration. Current Technical Specification 
    3.7.14 will ensure that an adequate spent fuel pool boron 
    concentration is maintained in the McGuire spent fuel storage pools. 
    A McGuire Station UFSAR change will revise Chapter 16, ``Selected 
    Licensee Commitments'', to provide for adequate monitoring of the 
    remaining Boraflex in the spent fuel pool racks. If that monitoring 
    identifies further reductions in the Boraflex panels which would not 
    support the conclusions of the McGuire Criticality Analysis, then 
    the McGuire TS's and design bases would be revised as needed to 
    ensure that acceptable subcriticality are maintained in the McGuire 
    spent fuel storage pools.
    
    Significant Change in Spent Fuel Pool Temperature
    
        There is no significant increase in the probability of either 
    the loss of normal cooling to the spent fuel pool water or a 
    decrease in pool water temperature from a large emergency makeup 
    when considering the degradation of the Boraflex in the spent fuel 
    pool racks and the presence of soluble boron in the pool water for 
    subcriticality control since a high concentration of soluble boron 
    has always been maintained in the spent fuel pool water. Current 
    Technical Specification 3.7.14 will ensure that an adequate spent 
    fuel pool boron concentration is maintained in the McGuire spent 
    fuel storage pools.
        A loss of normal cooling to the spent fuel pool water causes an 
    increase in the temperature of the water passing through the stored 
    fuel assemblies. This causes a decrease in water density that would 
    result in a decrease in reactivity when Boraflex neutron absorber 
    panels are present in the racks. However, since a reduction in the 
    amount of Boraflex present in the racks is considered, and the spent 
    fuel pool water has a high concentration of boron, a density 
    decrease causes a positive reactivity addition. However, the 
    additional negative reactivity provided by the current boron 
    concentration limit, above that provided by the concentration 
    required to maintain keff less than or equal to 0.95 
    (1170 ppm), will compensate for the increased reactivity which could 
    result from a loss of spent fuel pool cooling event. Because 
    adequate soluble boron will be maintained in the spent fuel pool 
    water, the consequences of a loss of normal cooling to the spent 
    fuel pool will not be increased. Current Technical Specification 
    3.7.14 will ensure that an adequate spent fuel pool boron 
    concentration is maintained in the McGuire spent fuel storage pools.
        A decrease in pool water temperature from a large emergency 
    makeup causes an increase in water density that would result in an 
    increase in reactivity when Boraflex neutron absorber panels are 
    present in the racks. However, the additional negative reactivity 
    provided by the current boron concentration limit, above that 
    provided by the concentration required to maintain keff 
    less than or equal to 0.95 (1170 ppm), will compensate for the 
    increased reactivity which could result from a decrease in spent 
    fuel pool water temperature. Because adequate soluble boron will be 
    maintained in the spent fuel pool water, the consequences of a 
    decrease in pool water temperature will not be increased. Current 
    Technical Specification 3.7.14 will ensure that an adequate spent 
    fuel pool boron concentration is maintained in the McGuire spent 
    fuel storage pools.
        2. Will the change create the possibility of a new or different 
    kind of accident from any previously evaluated?
        No. Criticality accidents in the spent fuel pool are not new or 
    different types of accidents. They have been analyzed in Section 
    9.1.2.3 of the Updated Final Safety Analysis Report and in 
    Criticality Analysis reports associated with specific licensing 
    amendments for fuel enrichments up to 4.75 weight percent U-235. 
    Specific accidents considered and evaluated include fuel assembly 
    drop, accidental misloading of spent fuel assemblies into the spent 
    fuel pool racks, and significant changes in spent fuel pool water 
    temperature. The accident analysis in the Updated Final Safety 
    Analysis Report remains bounding.
        The possibility for creating a new or different kind of accident 
    is not credible. The amendment proposes to take credit for the 
    soluble boron in the spent fuel pool water for reactivity control in 
    the spent fuel pool while maintaining the necessary margin of 
    safety. Because soluble boron has always been present in the spent 
    fuel pool, a dilution of the spent fuel pool soluble boron has 
    always been a possibility, however this accident was not considered 
    credible. For the proposed amendment, the spent fuel pool dilution 
    evaluation (Attachment 7) demonstrates that a dilution of the boron 
    concentration in the spent fuel pool water which could increase the 
    rack keff to greater than 0.95 (constituting a reduction 
    of the required margin to criticality) is not a credible event. The 
    requirement to maintain boron concentration in the spent fuel pool 
    water for reactivity control will have no effect on normal pool 
    operations and maintenance. There are no changes in equipment design 
    or in plant configuration. This new requirement will not result in 
    the installation of any new equipment or modification of any 
    existing equipment. Therefore, the proposed amendment will not 
    result in the possibility of a new or different kind of accident.
        3. Will the change involve a significant reduction in a margin 
    of safety?
        No. The proposed Technical Specification changes and the 
    resulting spent fuel storage operating limits will provide adequate 
    safety margin to ensure that the stored fuel assembly array will 
    always remain subcritical. Those limits are based on a plant
    
    [[Page 27319]]
    
    specific criticality analysis (Attachment 6) based on the 
    ``Westinghouse Spent Fuel Rack Criticality Analysis Methodology'' 
    described in Reference 1. The Westinghouse methodology for taking 
    credit for soluble boron in the spent fuel pool has been reviewed 
    and approved by the NRC (Reference 6). This methodology takes 
    partial credit for soluble boron in the spent fuel pool and requires 
    conformance with the following NRC Acceptance criteria for 
    preventing criticality outside the reactor:
        (1) keff shall be less than 1.0 if fully flooded with 
    unborated water which includes an allowance for uncertainties at a 
    95% probability, 95% confidence (95/95) level; and
        (2) keff shall be less than or equal to 0.95 if fully 
    flooded with borated water, which includes an allowance for 
    uncertainties at a 95/95 level.
        The criticality analysis utilized credit for soluble boron to 
    ensure keff will be less than or equal to 0.95 under 
    normal circumstances, and storage configurations have been defined 
    using a 95/95 keff calculation to ensure that the spent 
    fuel rack keff will be less than 1.0 with no soluble 
    boron. Soluble boron credit is used to provide safety margin by 
    maintaining keff less than or equal to 0.95 including 
    uncertainties, tolerances and accident conditions in the presence of 
    spent fuel pool soluble boron. The loss of substantial amounts of 
    soluble boron from the spent fuel pool which could lead to exceeding 
    a keff of 0.95 has been evaluated (Attachment 7) and 
    shown to be not credible. Accordingly, the required margin to 
    criticality is not reduced.
        The evaluations in Attachment 7, which show that the dilution of 
    the spent fuel pool boron concentration from the conservative 
    assumed initial boron concentration (2475 ppm) to the minimum boron 
    concentration required to maintain keff [less than or 
    equal to] 0.95 (440 ppm) is not credible, combined with the 95/95 
    calculation which shows that the spent fuel rack keff 
    will remain less than 1.0 when flooded with unborated water, provide 
    a level of safety comparable to the conservative criticality 
    analysis methodology required by References 2, 3 and 4.
        Therefore the proposed changes in this license amendment will 
    not result in a significant reduction in the plant's margin of 
    safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: J. Murray Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina.
    
        Attorney for licensee: Mr. Albert Carr, Duke Energy Corporation, 
    422 South Church Street, Charlotte, North Carolina.
    
        NRC Section Chief: Richard L. Emch, Jr.
    
    Duke Energy Corporation, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: April 6, 1999.
    
        Description of amendment request: The proposed amendments would 
    expand the allowable values for Interlocks P-6 (Intermediate Range 
    Neutron Flux) and P-10 (Power Range Neutron Flux) in TS 3.3.1, Table 
    3.3.1-1, Function 16, Reactor Trip System Interlocks, as recommended by 
    Westinghouse.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated; or (2) Create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated; or (3) Involve a significant reduction in a 
    margin of safety.
        Criterion 1--Would operation of the facility in accordance with 
    the requested amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The reactor protection interlocks are provided to ensure reactor 
    trips are in the correct configuration for the current unit status. 
    They back up operator actions to ensure protection system functions 
    are not bypassed during unit conditions under which the safety 
    analysis assumes the functions are not bypassed. The proposed 
    changes involve changing the lower value of the P-10 permissive 
    (power range (PR) neutron flux) allowable values from [greater than 
    or equal to] 9% RTP to [greater than or equal to] 7% RTP, and 
    changing the P-6 permissive (intermediate range (IR) neutron flux) 
    allowable value from [greater than or equal to] 6E11 amp to [greater 
    than or equal to] 4E-11 amp. Changing the P-10 allowable value would 
    allow for tripping and resetting of the permissive at a lower 
    reactor power level. Changing the P-6 allowable value would allow 
    the source range (SR) channels to be blocked at a lower increasing 
    reactor power level and delay resetting of the permissive at a lower 
    decreasing reactor power level.
        A review of the UFSAR Chapter 15 accident analyses determined 
    that no credit is taken for the SR reactor trip or the IR reactor 
    trip for any of the UFSAR accidents. Credit is taken for the PR low 
    setpoint trip for a feedwater system malfunction causing an increase 
    in feedwater flow accident (15.1.2), uncontrolled rod cluster 
    control assembly bank withdrawal from a subcritical or low power 
    startup condition accident (15.4.1), and spectrum of rod cluster 
    control assembly ejection accidents (15.4.8). All three of these 
    accident scenarios are bounded by cases at 0% RTP taking credit for 
    the PR low setpoint trip and cases at [greater than or equal to] 10% 
    RTP taking credit for the PR high setpoint trip. The uncontrolled 
    rod cluster control assembly bank withdrawal from power accident 
    (15.4.2) analyses are performed at initial power levels of 10%, 50%, 
    and 100% RTP to demonstrate that acceptable results are obtained for 
    a range of initial power levels. For this accident, the PR neutron 
    flux high setpoint trip, high pressurizer pressure trip, overpower 
    delta-T (OPDT) trip and overtemperature delta-T (OTDT) trip provide 
    core protection. With the P-10 reset function changed to as low as 
    7% RTP, the conclusions of Section 15.4.2 analysis would not change. 
    Since the uncontrolled bank withdrawal event is analyzed from both 
    zero power and 10% RTP, all low power initial conditions are 
    adequately bounded. Therefore, the proposed changes will not 
    increase the probability or consequences of an accident previously 
    evaluated.
        Criterion 2--Would operation of the facility in accordance with 
    the requested amendment create the possibility of a new or different 
    kind of accident from any previously evaluated?
        The proposed changes to the allowable values will provide 
    adequate deadbands between the trip and reset setpoints as well as 
    adequate margin for instrument drift. The reactor trip system 
    overpower trips continue to perform their safety function as assumed 
    in safety analyses. Only the permissives (P-6 and P-10) for blocking 
    and unblocking of overpower reactor trips are changed. The proposed 
    changes will not invalidate any of the UFSAR accident analyses. The 
    proposed changes will not introduce any new failure modes. 
    Therefore, the proposed changes will not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        Criterion 3--Would operation of the facility in accordance with 
    the requested amendment involve a significant reduction in a margin 
    of safety?
        The proposed changes involve lowering the Technical 
    Specification allowable values associated with the P-10 and P-6 
    permissives for blocking and unblocking of reactor overpower trips. 
    The lowering of these allowable values is not considered a 
    significant reduction since it is just enough to accommodate a 
    deadband recommended by Westinghouse and a margin for instrument 
    drift. The proposed changes will not invalidate any UFSAR Chapter 15 
    accident analyses. Therefore, the proposed changes will not involve 
    a significant reduction in a margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: J. Murrey Atkins Library,
    
    [[Page 27320]]
    
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina.
    
        Attorney for licensee: Mr. Albert Carr, Duke Energy Corporation, 
    422 South Church Street, Charlotte, North Carolina.
    
        NRC Section Chief: Richard L. Emch, Jr.
    
    Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of amendment request: April 26, 1999.
    
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications to provide a method for obtaining a 
    Nuclear Regulatory Commission review of (a) the analytical details 
    regarding a revised methodology for determining steam generator tube 
    loads following a main steam line break, and (b) the crediting of the 
    main steam line break detection and feedwater isolation instrumentation 
    as a means for providing runout protection for the turbine-driven 
    emergency feedwater pump.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        No. The proposed changes involve: (a) revising the methodology 
    utilized to determine steam generator tube loads following a main 
    steam line break (MSLB); and (b) utilizing the MSLB detection and 
    feedwater isolation instrumentation as an additional means of 
    providing runout protection of the turbine-driven emergency 
    feedwater (EFW) pump.
        The revised methodology utilized to determine steam generator 
    tube loads following a MSLB is consistent with the methodology 
    utilized in the MSLB containment response analysis which has 
    received Nuclear Regulatory Commission (NRC) approval. The revised 
    MSLB analysis reaches the same conclusion as the original analysis 
    (i.e., steam generator tube integrity is maintained). The new 
    analysis takes into consideration the operation of the MSLB 
    detection and feedwater isolation instrumentation to terminate main 
    feedwater (MFW) flow and inhibit the auto-start of or auto-stop the 
    turbine-driven EFW pump. This instrumentation is QA-1, whereas the 
    Integrated Control System (ICS) is non-safety. Furthermore, the 
    revised MSLB analysis results in a greater temperature difference 
    between the steam generator tube and shell, thus, more conservative 
    steam generator tube loads than those identified in the original 
    MSLB analysis.
        Also, in the event that the MSLB detection and feedwater 
    isolation instrumentation does not function properly, the non-safety 
    ICS is still available to maintain steam generator water level at 
    the post-trip minimum level as assumed in the original analysis.
        Currently, operator action is the only credited means to protect 
    the turbine-driven RFW pump from runout. The MSLB detection and 
    feedwater isolation instrumentation provides an additional method to 
    protect the turbine-driven EFW pump from runout. Crediting the MSLB 
    detection and feedwater isolation instrumentation simply adds 
    defense in depth.
        There are no physical changes to the plant structures, systems, 
    or components (SSCs) or operating procedures, nor are there any 
    changes to safety limits or set points. Also, no new radiological 
    release pathways are created.
        Thus, the proposed change does not significantly increase the 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from the accidents previously evaluated?
        No. The reanalysis of the steam generator tube loads following a 
    MSLB accident is limited to an accident that is already evaluated in 
    the UFSAR. The methodology is similar to the current analysis for 
    the MSLB containment response. The effects of the MSLB on steam 
    generator tube integrity are the same as in the original analysis--
    tube integrity is maintained.
        The revised analysis takes into consideration the operation of 
    the MSLB detection and feedwater isolation instrumentation, which 
    terminates MFW flow and inhibits the auto-start of or auto-stops the 
    turbine-driven EFW pump following a MSLB. As assumed in the original 
    analysis, the non-safety ICS will remain available to control steam 
    generator water level at the post-trip minimum level should a 
    malfunction occur in the MSLB detection and mitigation circuit. 
    Should this malfunction occur, the resulting tube stresses would 
    decrease relative to the revised analysis.
        Crediting the MSLB detection and feedwater isolation 
    instrumentation as a means to protect the turbine-driven EFW pump 
    from runout simply adds defense in depth.
        There are no physical changes to the plant SSCs or operating 
    procedures. There are no new hazardous materials or potential 
    missiles. It does not introduce the possibility of any new or 
    different malfunctions. No safety limits or set points are changed.
        Thus, the proposed change does not create the possibility of a 
    new or different kind of accident.
        3. Involve a significant reduction in a margin of safety?
        No. The reanalysis of the steam generator tube loads following a 
    MSLB accident is similar to the current analysis for the previously 
    NRC approved MSLB containment response. The conclusion of the 
    revised MSLB steam generator tube load analysis is the same as the 
    conclusion in the original analysis--steam generator tube integrity 
    is maintained.
        Crediting the MSLB detection and feedwater isolation 
    instrumentation as a means to protect the turbine-driven EFW pump 
    from runout simply adds defense in depth.
        There are no safety limit, set point, design parameters, or 
    operating procedure changes required. The integrity of the fuel 
    cladding, reactor coolant system, and containment are preserved.
        Thus, the proposed change does not involve a significant 
    reduction in a margin of safety.
        Duke has concluded based on the above information that there are 
    no significant hazards involved in this LAR.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
        Attorney for licensee: Anne W. Cottington, Winston and Strawn, 1200 
    17th Street, NW., Washington, DC.
    
        NRC Section Chief: Richard L. Emch, Jr.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: April 9, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise the requirements affecting the surveillance methods for the 
    containment tendons, the conduct of containment visual inspections, and 
    the reporting methods employed in disseminating the results of these 
    inspections to the Nuclear Regulatory Commission.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Criterion 1--Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The proposed change to the ANO-1 [Arkansas Nuclear One, Unit 1] 
    TS [Technical Specifications] replaces previous requirements and 
    commitments to establish a containment inspection program based on 
    the guidance provided in Regulatory Guide 1.35, Revision 2 in favor 
    of regulations depicted in [Title] 10 [of the] CFR [Code of
    
    [[Page 27321]]
    
    Federal Regulations] 50.55a(g)(6)(ii)(B) and 50.55a(b)(2)(ix). ANO-1 
    is implementing a containment inspection program to comply with 
    these new regulatory requirements. The final rule specifies 
    requirements to assure that the critical areas of the containment 
    structure are routinely inspected to detect and take corrective 
    action for defects that could compromise structural integrity.
        Maintaining reactor building structural integrity is independent 
    of the operation of the reactor coolant system (RCS), the reactor 
    protection system (RPS) and emergency core cooling system (ECCS). 
    The reactor building is not considered to be the initiator of any 
    accident previously evaluated. The physical location of inspection 
    details does not prevent or inhibit the reactor building from 
    functioning as designed to provide an acceptable barrier against 
    release of radioactive materials to the environment. Through 
    appropriate inspections and implementation of corrective actions for 
    any degradation discovered during the inspections that might lead to 
    containment structural failures, the probability or consequences of 
    accidents will not be increased.
        Therefore, the removal of inspection details from the TS does 
    not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        Criterion 2--Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        Maintaining containment structural integrity is independent of 
    the operation of the RCS, the RPS and ECCS. The proposed changes do 
    not change the design, configuration, or method of operation of the 
    plant. By implementing corrective actions for any degradation 
    discovered during the required inspections of the containment, the 
    possibility of a new or different kind of accident will not be 
    created. Implementation of the requirements of Subsection IWL of the 
    ASME [American Society of Mechanical Engineers] code and those of 10 
    CFR 50.55a(g)(6)(ii)(B) and 50.55a(b)(2)(ix) provide an equally 
    acceptable containment inspection program.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3--Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The removal of the level of detail currently found in the ANO-1 
    TS regarding reactor building inspections and incorporating the 
    applicable requirements of Subsection IWL of the ASME code and of 10 
    CFR 50.55a(g)(6)(ii)(B) and 50.55a(b)(2)(ix) into the ANO-1 
    containment inspection program has no impact on any safety analysis 
    assumptions. Requirements associated with containment inspections 
    are controlled by safety related procedure 5220.011. Sufficient 
    controls exist under the procedure change process at ANO-1 to ensure 
    current and future regulations and commitments are properly 
    addressed when making revisions to the containment inspection 
    procedure. The addition of structural integrity requirements to ANO-
    1 TS Specification 3.6.1 imposes consistent requirements with those 
    previously specified in the ANO-1 TSs. The containment inspection 
    program ensures that the containment will function as designed to 
    provide an acceptable barrier against release of radioactive 
    materials to the environment. Through the implementation of the 
    containment inspection program, the existing margin of safety is 
    preserved.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
    
        NRC Section Chief: Robert A. Gramm.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: April 9, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise the requirements associated with the station batteries and the 
    direct current (dc) sources to the 125 volt dc switchyard distribution 
    system.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Criterion 1--Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The switchyard 125V DC control power source requirements do not 
    meet the criteria for inclusion in Technical Specifications (TSs) as 
    evaluated with respect to the selection criteria of [Title] 10 [of 
    the] CFR [Code of Federal Regulations] 50.36. These control power 
    sources are not assumed to mitigate accident or transient events. 
    The effects of a loss of these control power sources are enveloped 
    by the Loss of Offsite Power (LOOP) event and relocation is 
    considered to have a non-significant impact on the probability or 
    severity of a LOOP event. These requirements will be relocated from 
    the TSs to an appropriate administratively controlled document and 
    maintained pursuant to 10 CFR 50.59.
        Proposed changes incorporating the requirements of TS 3.7.1.D, 
    3.7.2.E, 3.7.2.F, and 3.7.2.A, as related to the DC electrical power 
    subsystems, in the new TS 3.7.3 results in a more stringent 
    requirement for the ANO-1 [Arkansas Nuclear One, Unit 1] TSs in that 
    reductions to lower conditions of operation in shorter periods of 
    time are now required. These more stringent requirements are not 
    assumed to be initiators of any analyzed events and will not alter 
    assumptions relative to mitigation of accident or transient events.
        The proposed addition of TS 3.7.4 allowing continued operation 
    for a limited period of time with battery cell parameters not within 
    limits under certain conditions clarifies an allowance that 
    currently exists in the ANO-1 TS due to the absence of acceptance 
    criteria for the battery cell parameter surveillances.
        Proposed changes in Surveillance Requirements and Frequencies 
    reflect current industry guidance on maintenance and testing of the 
    station batteries. These requirements, in themselves, are not 
    considered to be initiators of any analyzed accident condition. 
    Although some frequencies have been extended, continued performance 
    of maintenance activities in accordance with IEEE-450 [Institute of 
    Electrical and Electronic Engineers, ``Recommended Practice for 
    Maintenance Testing and Replacement of Vented Lead-Acid Batteries 
    for Stationary Applications], in addition to the required 
    Surveillance Requirements, ensures that corrective maintenance can 
    be performed prior to a condition challenging an operability limit.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2--Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The proposed changes revise the surveillance requirements, and 
    required actions associated with the 125VDC distribution system and 
    the battery cell parameters. The requirements associated with the 
    ANO-1 switchyard DC sources have been relocated to licensee control. 
    The proposed changes do not change the design, configuration, or 
    method of operation of the plant.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3--Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        Relocation of the switchyard 125V DC control power source 
    requirements has no impact on any safety analysis assumptions. In 
    addition, the requirements associated with these control power 
    sources are relocated to an owner controlled document for which 
    future changes will be evaluated pursuant to the requirements of 10 
    CFR 50.59.
        Proposed changes incorporating the requirements of TS 3.7.1.D, 
    3.7.2.E, 3.7.2.F, and 3.7.2.A, as related to the DC electrical power 
    subsystems, in the new TS 3.7.3 impose more stringent requirements 
    than previously specified for ANO-1.
        The proposed addition of TS 3.7.4 allowing continued operation 
    for a limited period of time with battery cell parameters not within 
    limits under certain conditions clarifies an allowance that 
    currently exists in the ANO-1 TS due to the absence of acceptance 
    criteria for the battery cell parameter surveillances.
    
    [[Page 27322]]
    
        Proposed changes in Surveillance Requirements and Frequencies 
    reflect current industry guidance on maintenance and testing of the 
    station batteries. Although some frequencies have been extended, 
    continued performance of maintenance activities in accordance with 
    IEEE-450, in addition to the required Surveillance Requirements, 
    ensures that corrective maintenance can be performed prior to a 
    condition challenging an operability limit.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
    
        NRC Section Chief: Robert A. Gramm.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio
    
        Date of amendment request: March 17, 1999.
    
        Description of amendment request: The proposed amendment changes 
    the Perry Nuclear Power Plant as described in the Updated Safety 
    Analysis Report. The change incorporates a leak-off line in the 
    residual heat removal system. The leak-off line is designed to 
    eliminate an operator work around, which will significantly reduce the 
    collective dose to plant operations personnel.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed modification has been described, and will be 
    procured and installed in accordance with the original design codes 
    and standards. The safety functions of the RHR [residual heat 
    removal] system have not been impacted by the change. Systems 
    supporting the operation of the RHR system have not been affected by 
    this modification. Though the modification affects the Containment 
    System, the containment remains capable of performing its associated 
    safety functions to the same level as the original design.
        The accidents of concern are the Loss-Of-Coolant (LOCA) and the 
    Loss of Shutdown Cooling. The proposed change has been designed in 
    accordance with the original codes and standards. The proposed 
    change will not alter the operation of any plant equipment assumed 
    to function in response to the aforementioned analyzed events or 
    otherwise increase their failure probability. Therefore, the 
    probability of occurrence or the consequences of an accident 
    previously evaluated remains unchanged.
        2. The proposed change would not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed modification has been designed, and will be 
    procured and installed in accordance with the original RHR system 
    design codes and standards. RHR system functions have not been 
    impacted by the change. Systems supporting the operation of the RHR 
    system have not been affected. Failure of the modification to 
    perform its design function due to leak-off line failure or blockage 
    would be identical to the current RHR system performance. Improper 
    operation of the valves associated with the modification have been 
    evaluated and will not prevent or otherwise inhibit the RHR or 
    Containment systems from performing their applicable safety 
    functions.
        Missile generation is not a concern since no mechanisms 
    conducive to missile generation have been introduced. Electrical 
    analyses have shown there is no adverse effect upon the diesel 
    generator loadings. A single failure of the new configuration will 
    not result in more than the loss of a single RHR loop which is 
    already analyzed. Therefore, the possibility of a new or different 
    kind of accident from any previously evaluated has not been created.
        3. The proposed change will not involve a significant reduction 
    in the margin of safety.
        The proposed modification has been designed, and will be 
    procured and installed in accordance with the original RHR system 
    design codes and standards. The RHR and Containment systems remain 
    capable of performing their safety functions. Systems supporting the 
    operation of the RHR system have not been affected. Hence, the RHR 
    system margin of safety with respect to safety classification, 
    protection, redundancy, and seismic classification remains 
    unaffected.
        The margins of safety contained in the Technical Specifications 
    and the associated Bases also remain unaffected by this 
    modification. Specifically, Technical Specifications 3.4.6, 
    ``Reactor Coolant System Pressure Isolation Valve Leakage'; 3.4.9, 
    ``RHR Shutdown Cooling System--Hot Shutdown'; 3.4.10, ``RHR Shutdown 
    Cooling System--Cold Shutdown'; 3.6.2.1, ``Suppression Pool Average 
    Temperature'; and 3.6.2.2, ``Suppression Pool Water Level'; and the 
    associated Bases remain unchanged and fully applicable. Hence, the 
    margins of safety defined in the Technical Specifications remains 
    unaffected.
        Therefore, the proposed modification does not involve a 
    significant reduction in the margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
    
        NRC Section Chief: Anthony J. Mendiola.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: March 31, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to (1) increase the minimum reactor 
    coolant system (RCS) flow rate limit, (2) delete the reactor coolant 
    flow rate footnote, and (3) change the minimum frequency surveillance 
    for RCS flow rate.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Combustion Engineering (ABB/CE) in Thermal-Hydraulic Report CR-
    94-19-CSE95-1131, Revision 0 performed a comprehensive evaluation of 
    the effects the removal of the orifice plates would have on steam 
    generator tube degradation. It was concluded that the removal of the 
    orifice plates would increase the primary flow rate by approximately 
    5%.
        The removal of the orifice plates was estimated to increase the 
    probability of tubes requiring repair over the lifetime of the 
    plant. However, the presence of the orifice plates had prevented 
    inspection of approximately 22% of the steam generator tubes for 
    circumferential cracks on the hot-leg side. Therefore, it was 
    concluded that the removal of the orifice plates did not increase 
    the probability of steam generator tube failure, given that the 
    tubes previously covered by the plates are now inspected each outage 
    in accordance with the Electrical Power Research Institute 
    Pressurized Water Reactor (EPRI PWR) steam generator examination 
    guidelines. Fort Calhoun Station is using the eddy current 
    inspection technology to ensure that tubes showing evidence of a 
    crack exceeding the present plugging criteria will be repaired or 
    removed from service. Industry experience has shown that even in 
    cases of severely degraded tubes, the
    
    [[Page 27323]]
    
    resulting primary to secondary leak rates are insignificant compared 
    to those analyzed in the design basis steam generator tube rupture 
    event.
        Calculation of the Reactor Coolant Flow Rate using the heat 
    balance methodology once every refueling outage is consistent with 
    requirements contained in the NUREG 1432, Improved Technical 
    Specifications for Combustion Engineering Plants' surveillance 
    requirement 3.4.1.4.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The original orifice plates were installed on each steam 
    generator hot leg tube sheet in the primary inlet plenum as a field 
    modification prior to the initial fuel load in the year 1973. The 
    orifice plates were designed to increase the hydraulic resistance of 
    the primary coolant flow rate in the associated tubes, thereby 
    reducing the primary coolant temperature inside the tubes. Reduction 
    of the primary coolant temperature and flow rate would decrease the 
    heat flux, thus improving the steam quality and reducing the 
    potential for dry-out and surface deposits on the outer surface of 
    the tubes. However, due to inaccessibility, these originally 
    installed orifice plates had prevented tube inspection in the hot 
    leg tube sheet area, even with the latest state-of-the-art eddy 
    current probe technology. The orifice plates also prevented normal 
    repair techniques such as steam generator tube plugging and 
    sleeving.
        The original orifice plates were removed during the 1996 
    refueling outage. However, there were concerns related to 
    Westinghouse fuel failures as a result of flow-induced vibration. To 
    address those concerns, new ``removable'' orifice plates were 
    installed to maintain the RCS flow rate at the previous level. Since 
    then, the remaining batches of the Westinghouse fuel considered most 
    susceptible to flow-induced vibration were replaced during the 1998 
    refueling outage, thus minimizing the concerns and allowing the 
    permanent removal of the ``removable'' orifice plates.
        The removal of the ``removable'' orifice plates returned the 
    steam generators to their original design configuration. RCS flow 
    rate has increased by virtue of decreased hydraulic resistance 
    through the steam generators. No other systems or components other 
    than the steam generators have been affected. The resulting change 
    in operational parameters (decreased reactor coolant Thot 
    temperature and increased flow rate) has been evaluated for the 
    Updated Safety Analysis Report Chapter 14. Potential adverse 
    consequences of the modifications were (1) increase in reactor 
    vessel component vibration, (2) increase in hydraulic loading, and 
    (3) increase in steam generator tube degradation for row 1-18 tubes. 
    The potential adverse consequences were evaluated and found to be 
    acceptable.
        Calculation of the Reactor Coolant Flow Rate using the heat 
    balance methodology once every refueling outage is consistent with 
    requirements contained in the NUREG 1432, Improved Technical 
    Specifications for Combustion Engineering Plants' surveillance 
    requirement 3.4.1.4.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The removal of the orifice plates has resulted in approximately 
    a 5% increase in the reactor coolant flow rate. This has increased 
    the margin for minimum reactor coolant system flow rate specified in 
    Technical Specifications Section 2.10.4, Power Distribution Limits, 
    Item (5), DNBR Margin During Power Operation Above 15% of Rated 
    Power. Steam Generator tube inspections performed in accordance with 
    Technical Specifications Section 3.17, Steam Generator Tubes, have 
    not been adversely affected.
        The increased flow rate has been analyzed for the thermal 
    hydraulic effects on the reactor core and was found acceptable.
        Calculation of the Reactor Coolant Flow Rate using the heat 
    balance methodology once every refueling outage is consistent with 
    requirements contained in the NUREG 1432 [Improved Technical 
    Specifications for Combustion Engineering Plants] surveillance 
    requirement 3.4.1.4.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
    
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
    
        NRC Project Director: Stuart A. Richards.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: January 28, 1999.
    
        Description of amendment request: This application for amendment to 
    the Indian Point 3 (IP3) Technical Specifications (TSs) proposes to 
    remove two lists of Containment Isolation Valves (CIVs) in Tables 3.6-1 
    and 4.4-1 and make related changes to TSs 1.10, 3.6.A.1, and 4.4 and 
    the associated bases.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        Response: No. Operation of Indian Point 3 in accordance with the 
    proposed license amendment does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The removal of the two component listings (i.e., Tables 
    3.6-1 and 4.4-1) and the TS references to them from the TS requested 
    by this submittal is performed in accordance with the guidance 
    provided by the NRC in GL 91-08 [Generic Letter 91-08]. As 
    established by the NRC, in the aforementioned GL, such a change will 
    not alter existing TS requirements or those components to which they 
    apply. Required information contained in the two tables being 
    removed is duplicated in the FSAR [final safety analysis report] and 
    other appropriate plant procedures. Any subsequent changes regarding 
    the individual components (i.e., the containment isolation valves) 
    or their operation (e.g., valve positioning under administrative 
    controls) would be addressed in accordance with the requirements 
    specified in the Administrative Controls section of the TS regarding 
    changes to plant procedures and/or changes to the FSAR (i.e., 10 CFR 
    50.59). These changes will not alter any structure, system, or 
    component and, therefore, will not result in the possibility of an 
    increase in [the] probability or consequence of an accident 
    previously evaluated.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response: No. The proposed changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated. The deletion of two component listings (i.e., Tables 3.6-
    1 and 4.4-1) and the TS references to them from the Technical 
    Specifications and the removal of all references made in the TS 
    regarding these two listings will not alter how the individual 
    components (i.e.--the containment isolation valves) identified in 
    the tables are designed, operated, tested, or maintained. Testing of 
    CIVs will be performed as required by 10 CFR part 50, Appendix J and 
    IP3 TS 6.14.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response: No. The proposed license amendment does not involve a 
    significant reduction in a margin of safety. The proposed changes 
    are in accordance with recommendations provided by NRC in Generic 
    Letter 91-08 and the Standard Technical Specifications, NUREG 1431. 
    These changes will maintain current safety margins while reducing 
    the regulatory/administrative burdens to both the NRC and to the 
    Power Authority. As stated, the changes will not result in changes 
    to the design, operation, or maintenance of the ClVs, and the 
    testing of the CIVs will be in accordance with 10 CFR 50 Appendix J 
    and IP3 TS 6.14.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request
    
    [[Page 27324]]
    
    involves no significant hazards consideration.
    
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
    
        Attorney for licensee: Mr. David E. Blabey, 10 Columbus Circle, New 
    York, New York 10019.
    
        NRC Section Chief: S. Singh Bajwa.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: April 12, 1999.
    
        Description of amendment request: This application for amendment to 
    the Indian Point 3 (IP3) Technical Specifications (TSs) proposes to 
    remove the footnote restriction found on page 3.1-36 which states that 
    the departure from nucleate boiling (DNB) analysis contains adequate 
    margin for Cycle 10, but needs to be reviewed/approved prior to Cycle 
    11.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed?
        Response: The proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed. The removal of the footnote on TS page 3.1-36 
    is an administrative change in that it does not affect the DNB 
    limits of the current TS. The footnote was added to the TS as part 
    of Amendment 175, which permitted the use of V+ fuel at IP3. The 
    footnote required the Authority to demonstrate that sufficient DNB 
    margin existed for Cycle 11, prior to achieving criticality for that 
    cycle. The NRC requested this DNB limitation because the 
    applicability of the WRB-1 correlation to predict DNB performance 
    for the V+ fuel had not been adequately proven by fuel tests. 
    Westinghouse has completed fuel tests which verify that the use of 
    the WRB-1 correlation with the 15  x  15 V+ fuel is conservative. 
    Therefore, this DNB limitation is no longer applicable and the 
    footnote can be removed.
        2. Does the proposed license amendment create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated?
        Response: The proposed change does not create the possibility of 
    a new or different kind of accident, as the removal of the footnote 
    on TS page 3.1-36 does not affect the current TS DNB limits, plant 
    equipment, or the way the plant is operated. This footnote was 
    inserted into the TS as part of Amendment 175, which permitted the 
    use of 15  x  15 V+ fuel at IP3. Westinghouse had used scaling 
    techniques to demonstrate that the WRB-1 correlation correctly 
    predicted the critical heat flux performance of the 15  x  15 V+ 
    fuel. Since no fuel tests had been performed on this fuel design, 
    the NRC was concerned that the use of this correlation may be 
    unconservative. Therefore, approval to use the V+ fuel at IP3 was 
    granted based upon the DNB margin available during Cycle 10. This 
    limitation was contained in the footnote on TS page 3.1-36. 
    Westinghouse has recently completed fuel tests on 15  x  15 V+ fuel 
    which verify that the use of the WRB-1 correlation is conservative. 
    Therefore, the use of V+ fuel at IP3 is no longer dependent on the 
    amount of DNB margin available and the footnote can be removed.
        3. Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response: The proposed deletion of the footnote on TS page 3.1-
    36 does not involve a significant reduction in a margin of safety. 
    The footnote was introduced as part of Amendment 175, which 
    permitted the use of V+ fuel at IP3. The footnote required the 
    Authority to demonstrate that sufficient DNB margin existed for 
    Cycle 11, prior to achieving criticality for that cycle. The NRC 
    requested this DNB limitation because the applicability of the WRB-1 
    correlation to predict DNB performance for the V+ fuel had not been 
    adequately proven by fuel tests. Westinghouse has completed fuel 
    tests which verify that the use of the WRB-1 correlation with the 15 
     x  15 V+ fuel is conservative. Therefore, this DNB limitation is no 
    longer applicable and the footnote can be removed. The removal of 
    the footnote is an administrative change as deleting it does not 
    alter the current DNB margin or future DNB margins.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
    
        Attorney for licensee: Mr. David E. Blabey, 10 Columbus Circle, New 
    York, New York 10019.
    
        NRC Section Chief: S. Singh Bajwa.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of amendment request: March 29, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) by relocating the procedural 
    details of the Radiological Effluent Technical Specifications (RETS) to 
    the Offsite Dose Calculation Manual (ODCM). The TSs would also be 
    revised to relocate procedural details associated with solid 
    radioactive wastes to the Process Control Program (PCP). In addition, 
    the Administrative Controls section of the TSs would be revised to 
    incorporate programmatic controls for radioactive effluents and 
    environmental monitoring. The proposed changes are consistent with the 
    guidance provided in Generic Letter 89-01, ``Implementation of 
    Programmatic Controls for Radiological Effluent Technical 
    Specifications in the Administrative Controls Section of the Technical 
    Specifications and the Relocation of Procedural Details of RETS to the 
    Offsite Dose Calculation Manual or to the Process Control Program.''
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed changes do not affect accident initiators or 
    precursors and do not alter the design assumptions, conditions, 
    configuration of the facility or the manner in which the plant is 
    operated. The proposed changes do not alter or prevent the ability 
    of structures, systems, or components to perform their intended 
    function to mitigate the consequences of an initiating event within 
    the acceptance limits assumed in the Updated Final Safety Analysis 
    Report (UFSAR). The proposed changes are administrative in nature 
    and do not change the level of programmatic controls and procedural 
    details relative to radiological effluents.
        Implementation of programmatic controls for RETS in TS will 
    assure that the applicable regulatory requirements pertaining to the 
    control of radioactive effluents will continue to be maintained. 
    Since there are no changes to previous accident analysis, the 
    radiological consequences associated with these analyses remain 
    unchanged, therefore, the proposed changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not alter the design assumptions, 
    conditions, configuration of the facility or the manner in which the 
    plant is operated. The proposed changes have no impact on component 
    or system interactions. The proposed changes are administrative in 
    nature and do not change the level of programmatic controls and 
    procedural details relative to radiological
    
    [[Page 27325]]
    
    effluents. Therefore, these changes will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        (3) The proposed change does not involve a significant reduction 
    in a margin of safety.
        There is no impact on equipment design or operation and there 
    are no changes being made to the TS required safety limits or safety 
    system settings that would adversely affect plant safety as a result 
    of the proposed changes. The proposed changes are administrative in 
    nature and do not change the level of programmatic controls and 
    procedural details relative to radiological effluents. A comparable 
    level of administrative control will continue to be applied to those 
    design conditions and associated surveillances being relocated to 
    the ODCM or PCP. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
    
        NRC Section Chief: James W. Clifford.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: April 29, 1999 (TS 99-04).
    
        Description of amendment request: The proposed amendment would 
    change the Technical Specifications (TS) for Sequoyah (SQN) Units 1 and 
    2 by deleting the Auxiliary Feedwater (AFW) suction pressure low 
    channel functional surveillance test. The licensee's analysis of the 
    performance history revealed that the monthly functional test of this 
    instrument channel does not provide an increased assurance of 
    operability that justifies the monthly 7 hours per unit system 
    unavailability that it creates.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The probability of occurrence or the consequences for an 
    accident is not increased by this request. The proposal to delete 
    the monthly channel functional test for the auxiliary feedwater 
    (AFW) suction pressure low functions does not alter the way any 
    structure, system or component functions, does not modify the manner 
    in which the plant is operated, and reduces equipment out-of-service 
    time. This request does not degrade the ability of AFW to perform 
    its intended function. Therefore, the pressure switches will be 
    available to perform their intended function.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        A possibility for an accident or malfunction of a different type 
    than any evaluated previously in SQN's FSAR [Final Safety Analysis 
    Report] is not created. The proposal does not alter the way any 
    structure, system or component functions and does not modify the 
    manner in which the plant is operated. Therefore, the possibility of 
    a new or different kind of accident previously evaluated is not 
    created by the proposed change to delete the monthly functional test 
    of the AFW pressure switches.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The margin of safety has not been reduced since the test 
    methodologies are not being changed. Increasing the surveillance 
    interval does not change the results of accident analysis by this 
    request. The proposed change to delete the AFW system pressure low 
    channel functional test does not involve a significant reduction in 
    the margin of safety. The new frequency will not reduce the 
    reliability of the system and increases overall system availability. 
    Therefore, changing the frequency of the surveillance does not 
    reduce the margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 3740.
    
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H Knoxville, Tennessee 37902.
    
        NRC Section Chief: Sheri Peterson.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: April 29, 1999 (TS 99-03).
    
        Description of amendment request: The proposed amendment would add 
    new actions to Technical Specification (TS) Limiting Condition for 
    Operations (LCOs) 3.3.3.1 and 3.7.7 to address the situation when one 
    channel of radiation monitoring control room emergency ventilation 
    system actuation equipment is inoperable and would expand the mode of 
    applicability for LCOs 3.3.3.1 and 3.7.7 to include periods when 
    movement of irradiated fuel assemblies are involved and defines actions 
    to take in these instances.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed revision does not change any plant functions or 
    equipment operating practices for the radiation monitoring system 
    and control room emergency ventilation system (CREVS). The radiation 
    monitoring instruments and the CREVS are not considered to be the 
    source of any accident evaluated in the Final Safety Analysis 
    Report. These features provide accident mitigation functions that 
    will be utilized in response to postulated accident conditions. The 
    activities and failures that could contribute to the initiation of 
    an accident are not affected by the implementation of this revision. 
    This revision provides for more stringent requirements for operation 
    of the facility (additional limiting condition for operation [LCO] 
    actions and applicability requirements). Therefore the proposed 
    activity will not increase the probability of an accident.
        The proposed activity does not affect accident mitigation 
    capabilities or the radiation release amounts for postulated 
    accidents. This TS change will not affect requirements that the 
    radiation monitoring system and CREVS be maintained to support 
    accident mitigation. The functions and testing will remain the same 
    while operability requirements will become more stringent. This TS 
    change enhances the requirements associated with CREVS and the 
    initiation of this system such that inoperabilities are 
    appropriately handled to reduce the safety impact of component 
    inoperabilities. Therefore, the proposed change will not increase 
    the consequences of an accident and could reduce the consequences by 
    limiting operation with inoperable components and requiring the 
    application of appropriate actions for all conditions that could 
    result in a postulated accident that CREVS was designed to mitigate.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change provides more stringent operating 
    requirements for operation of the facility. The proposed
    
    [[Page 27326]]
    
    activity will not change any plant function or operating practice 
    that could impact accident initiators. Therefore, these more 
    stringent requirements do not result in operation that will increase 
    the probability of any postulated accidents. In addition, CREVS and 
    the associated actuation features are not considered to be the 
    source of an accident. Therefore, the proposed activity will not 
    create the possibility of an accident of a different kind.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed activity does not impact plant setpoints designed 
    to maintain the assumptions in the safety analysis or limits for the 
    actuation of systems to mitigate accidents. Plant functions and 
    operating practices will not be altered by the implementation of 
    more stringent requirements for operation of the facility. These 
    requirements, by definition, provide additional restrictions to 
    enhance plant safety. Therefore, the proposed activity will not 
    reduce the margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
    
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H Knoxville, Tennessee 37902.
    
        NRC Section Chief: Sheri Peterson.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: February 1, 1999, as supplemented on 
    April 19 and April 23, 1999.
    
        Description of amendment request: The amendment request proposes a 
    total replacement of current Technical Specifications Section 6, 
    ``Administrative Controls.'' Administrative changes to certain other 
    sections of Technical Specifications are also being made to conform to 
    the changes resulting from the re-write of Section 6.
    
        The proposed changes represent a comprehensive upgrade of Section 6 
    of the Vermont Yankee Technical Specifications, incorporating 
    improvements in content and format based on industry standards. In 
    accordance with industry practice some Technical Specifications 
    requirements are being relocated to the recently implemented Vermont 
    Yankee Technical Requirements Manual (TRM), Offsite Dose Calculation 
    Manual (ODCM), or Vermont Yankee Operational Quality Assurance Manual 
    (VOQAM) and will be eliminated from the Technical Specification upon 
    NRC approval.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:
        The proposed changes have no effect on plant hardware, plant 
    design, safety limit setting, or plant system operation and 
    therefore do not modify or add any initiating parameters that would 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        No new modes of operation are introduced by the proposed changes 
    such that additional adverse consequences would result. Accordingly, 
    the consequences of previously analyzed accidents are not 
    deleteriously affected by this proposed license amendment.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated, because:
        The proposed changes do not involve any physical alteration of 
    the plant (no new or different type of equipment will be installed) 
    or any change in the methods governing normal plant operation. These 
    changes do not affect the operation of any systems or components, 
    nor do they involve any potential initiating events that would 
    create any new or different kind of accident. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated for VYNPS.
        3. Involve a significant reduction in a margin of safety, 
    because:
        The proposed changes have no impact on any safety analysis 
    assumptions. Consequently, no margin of safety as described in the 
    Final Safety Analysis Report and defined in the basis of any 
    Technical Specification is reduced as a result of these changes.
        These proposed changes do not detrimentally affect the ability 
    of structures, systems and components important to safety to fulfill 
    their intended safety functions. Therefore, it is concluded that the 
    proposed changes do no[t] involve a significant reduction in a 
    margin of safety.
    
    Additional Safety Considerations for Specific Changes Deemed to be 
    ``Less Restrictive''
    
        In accordance with the criteria set forth in 10 CFR 50.92, Vermont 
    Yankee has evaluated the proposed changes to the [Vermont Yankee 
    Nuclear Power Station] VYNPS Technical Specifications and determined 
    that they do not involve a significant hazards consideration. Those 
    changes which are deemed to be ``less restrictive'' have been subject 
    to the following additional consideration:
    
        (a) Changes which are deemed to be ``less restrictive'' based 
    solely upon removal from the Technical Specifications and relocated 
    in VYNPC-controlled documents:
        NRC's Technical Specifications Branch has conducted reviews of 
    the Administrative Controls section of Standard Technical 
    Specifications and concluded that certain provisions historically 
    contained in Technical Specifications can be relocated to other 
    licensee documents for which changes to those provisions are 
    adequately controlled by other regulatory requirements. In general, 
    Administrative Controls are those requirements not covered by other 
    Technical Specifications, but are considered necessary to assure 
    operation of the facility in a safe manner. Application of this 
    criterion can be based on two categories or requirements: (a) 
    requirements not covered by other regulatory requirements, but are 
    considered necessary to assure the safe operation of the facility or 
    (b) specific requirements that are broadly covered by regulations or 
    other regulatory controls, for which details need to be specified in 
    the Technical Specifications to ensure safe plant operation. In 
    general, however, Technical Specifications need not duplicate other 
    regulatory requirements.
        As identified in Attachment A hereto, certain portions of the 
    current Technical Specifications are to be relocated to the 
    Technical Requirements Manual (TRM), Offsite Dose Calculation Manual 
    (ODCM), or the Vermont Yankee Operational Quality Assurance Manual 
    (VOQAM) and removed from the Technical Specifications. As an initial 
    step in this process, the subject requirements are being duplicated 
    in the TRM, ODCM, or VOQAM. Removal from the Technical 
    Specifications will occur upon NRC approval. The ability to relocate 
    these requirements is based on regulations and standards that 
    contain these provisions such that duplication in the Technical 
    Specifications is not necessary.
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:]
        The TRM is a[n] FSAR level document and is incorporated by 
    reference into the FSAR. Changes to the TRM will be strictly 
    controlled by the 10 CFR 50.59 process to ensure that proper reviews 
    are conducted. The relocation of requirements to the VYNPC-
    controlled TRM will not diminish the effectiveness of compliance 
    withthe relocated provisions. Since any changes to the TRM will be 
    evaluated per the requirements of 10 CFR 50.59, no increase 
    (significant or insignificant) in the probability or consequences of 
    an accident previously analyzed will be allowed. Therefore, these 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Changes to the ODCM are controlled by current Technical 
    Specifications and require the reporting to the NRC of changes to 
    the
    
    [[Page 27327]]
    
    ODCM with sufficient information to support the changes together 
    with appropriate analyses or evaluations justifying the changes. The 
    relocation of these details to the ODCM is thus acceptable 
    considering the controls provided by existing regulations and the 
    controls remaining in Technical Specifications for ODCM changes. 
    Therefore, these changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Relocation of the Technical Specification Administrative 
    Controls related to quality assurance from the Technical 
    Specifications to the VOQAM is consistent with the guidance provided 
    by the NRC in Administrative Letter 95-06, ``Relocation of Technical 
    Specification Administrative Controls Related to Quality 
    Assurance.'' Changes to the VOQAM are subject to the change control 
    process in 10CFR50.54(a). These provisions are adequate to ensure 
    that quality assurance program commitments are not reduced without 
    prior NRC approval. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, because:]
        The proposed changes do not involve any physical alteration of 
    the plant (no new or different type of equipment will be installed) 
    or a change in the methods governing normal plant operation. The 
    proposed change will not impose or eliminate any requirements, and 
    adequate control of the information will be maintained. Thus, this 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        [3. Involve a significant reduction in a margin of safety, 
    because:]
        The proposed changes will not reduce a margin of safety because 
    they have no impact on any safety analysis assumption. In addition, 
    the details to be transposed from the Technical Specifications to 
    the TRM, ODCM, and VOQAM are the same as the existing Technical 
    Specifications. Since any future changes to these provisions in the 
    TRM will be evaluated per the requirements of 10CFR50.59 and 
    Technical Specifications already requires supporting information be 
    submitted to the NRC for ODCM changes, no reduction (significant or 
    insignificant) in a margin of safety will be allowed. The provisions 
    of 10CFR50.54(a) are adequate to control changes to the VOQAM and 
    maintain current margins of safety.
        Based on 10CFR50.92, the existing requirement for NRC review and 
    approval of revisions (to the Technical Specifications provisions 
    proposed for relocation) does not have a specific margin of safety 
    upon which to evaluate. However, since the proposed changes are 
    consistent with industry standards, approved by the NRC, revising 
    the Technical Specifications to relocate these provisions will not 
    diminish administrative controls necessary to assure the safe 
    operation of the facility.
        (b) Change [9] identified in Attachments A and D [of the 
    February 1, 1999, submittal]:
        This change proposes to relax the requirement to have an 
    individual qualified in radiation protection procedures onsite at 
    all times. The proposed change will allow the position to be vacant 
    for up to two hours in order to provide for unexpected absence.
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:]
        The proposed change does not affect the probability of an 
    accident. The actions of an individual qualified in radiation 
    protection procedures are not assumed to be an initiator of an 
    accident. Also, the consequences of an accident are not affected by 
    the presence of an individual qualified in radiation protection 
    procedures. This proposed change does not impact the assumptions of 
    any design basis accident. This change will not alter assumptions 
    relative to the mitigation of an accident or transient event. This 
    change will not have any impact on the safe operation of the plant 
    because the presence of a person qualified in radiation protection 
    procedures is not required for the mitigation of any accident. 
    Therefore, this change will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, because:]
        This change will not physically alter the plant (no new or 
    different type of equipment will be installed). The changes in 
    methods governing normal plant operation are consistent with the 
    current safety analysis assumptions. Therefore, this change will not 
    create the possibility of a new or different type of accident from 
    any accident previously evaluated.
        [3. Involve a significant reduction in a margin of safety, 
    because:]
        The margin of safety is not affected by the presence or absence 
    onsite of an individual qualified in radiation protection 
    procedures. This proposed change has no effect on the assumptions of 
    any design basis accident. This change has no impact on the safe 
    operation of the plant since the presence onsite of an individual 
    qualified in radiation protection procedures is not required for the 
    mitigation of an accident. This change does not affect any plant 
    equipment or requirements for maintaining plant equipment. The 
    safety analysis assumptions will still be maintained, thus no 
    question of safety exists. Therefore, this change does not involve a 
    significant reduction in a margin of safety.
        (c) Change [10] identified in Attachments A and D [of the 
    February 1, 1999, submittal]:
        This change proposes to incorporate the allowances of a 
    temporary deviation from the shift staffing levels of 
    10CFR50.54(m)(2)(i) for up to two hours. In addition, this change 
    proposes to apply these same allowances to the positions of Shift 
    Engineer and non-licensed operators.
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:]
        The proposed change does not affect the probability of an 
    accident. The shift staffing level requirements are not assumed to 
    be an initiator or any analyzed event. Also, the consequences of an 
    accident are not affected by these temporary deviations to the shift 
    staffing levels. This proposed change does not impact the 
    assumptions of any design basis accident. This change will not alter 
    assumptions relative to the mitigation of an accident or transient 
    event, since 10CFR50.54(m) (ii) and (iii) still maintain the 
    requirements for the presence of licensed operators and senior 
    operators. This change has no impact on the safe operation of the 
    plant. The level of shift staffing will still be maintained as 
    required by 10CFR50.54(m) (ii) and (iii) and does not affect any 
    plant equipment or requirements for maintaining plant equipment. The 
    temporary deviations from the shift staffing level for up to two 
    hours to provide for unexpected absence, provided immediate action 
    is taken to fill the required position is acceptable in terms of 
    staffing requirements for the mitigation of an accident due to the 
    low probability of an accident occurring during these short-term, 
    infrequent deviations and the remaining licensed operators and 
    senior operators. Therefore, this change will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, because:]
        This change will not physically alter the plant (no new or 
    different type of equipment will be installed). The temporary 
    deviations from shift staffing levels are consistent with the 
    current safety analysis assumptions. Therefore, this change will not 
    create the possibility of a new or different type of accident from 
    any accident previously evaluated.
        [3. Involve a significant reduction in a margin of safety, 
    because:]
        The margin of safety in not reduced by allowing these temporary 
    deviations from shift staffing levels due to unforeseen events. This 
    proposed change has no effect on the assumptions of any design basis 
    accident. This change has no impact on the safe operation of the 
    plant since 10CFR50.54(m) (ii) and (iii) still maintain the 
    requirements for the minimum number of licensed operators and senior 
    operators necessary to safely operate the plant. This change does 
    not affect any plant equipment or requirements for maintaining plant 
    equipment. The safety analysis assumptions will still be maintained, 
    thus no question of safety exists. Therefore, this change does not 
    involve a significant reduction in a margin of safety.
        (d) Changes [38] and [39] identified in Attachments A and D [of 
    the February 1, 1999, submittal]:
        In accordance with 10CFR20.1601 (c), these changes propose 
    alternative methods for controlling access to high radiation areas 
    consistent with the intent of 10CFR20.1601 (a) and (b).
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:]
        The proposed changes do not affect the probability of an 
    accident. The controls used for access to high radiation areas are 
    not assumed in the initiation of any analyzed event. Also, the 
    consequences of an accident are not affected by these changes. These 
    changes are both consistent with good
    
    [[Page 27328]]
    
    radiological practices and will provide an adequate level of 
    radiation protection. These proposed changes do not impact the 
    assumptions of any design basis accident. These changes will not 
    alter assumptions relative to the mitigation of an accident or 
    transient event. These changes have no impact on safe operation of 
    the plant. Therefore, these changes will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, because:]
        The proposed changes will not create the possibility of an 
    accident. These changes will not physically alter the plant (no new 
    or different type of equipment or system will be installed). The 
    changes in methods governing normal plant operations are consistent 
    with the current safety analysis assumptions and deal only with 
    personnel exposure to radiation, not reactor safety. Therefore, 
    these changes will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        [3. Involve a significant reduction in a margin of safety, 
    because:]
        The margin of safety is not reduced due to these proposed 
    changes. These changes are both consistent with good radiological 
    safety practice and have been found to provide adequate levels of 
    radiation protection. In addition, these changes provide the benefit 
    of ensuring radiation dose to workers can be minimized by providing 
    the flexibility to select the best means of providing access control 
    to a high radiation area, given the plant area and radiological 
    conditions. These proposed changes have no impact on the safe 
    operation of the plant. No change in analytic limits or setpoints is 
    introduced by these changes. The safety analysis assumptions will 
    still be maintained, thus no question of nuclear safety exits. 
    Therefore, these changes do not involve a significant reduction in a 
    margin of safety.
        (e) Change [49] identified in Attachments A and D [of the 
    February 1, 1999, submittal]:
        This change proposes to relax the requirement for submitting the 
    (now-named) Occupational Radiation Exposure Report from the 
    currently required date of March 1 to April 30 of each year. April 
    30 is now the industry standard date for submittal of such reports.
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:]
        The proposed change does not affect the probability of an 
    accident. The submittal date of the Occupational Radiation Exposure 
    Report is not assumed to be an initiator of any analyzed event. 
    Also, the consequences of an accident are not affected by the 
    submittal date of this report. This proposed change does not impact 
    the assumptions of any design basis accident. This change will not 
    alter assumptions relative to the mitigation of an accident or 
    transient event. This change has no impact on the safe operation of 
    the plant. The report will still be required to be submitted each 
    year and does not affect any plant equipment or requirements for 
    maintaining plant equipment. The submittal date of this report is 
    not required for the mitigation of any accident. Therefore, this 
    change will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, because:]
        The proposed change will not create the possibility of an 
    accident. This change will not physically alter the plant (no new or 
    different type of equipment will be installed). The change in method 
    governing submittal of this report does not affect current safety 
    analysis assumptions. Therefore, this change will not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
        [3. Involve a significant reduction in a margin of safety, 
    because:]
        The margin of safety i[s] not reduced by allowing the report to 
    be submitted 60 days later. This proposed change has no effect on 
    the assumptions of the design basis accident. This change has no 
    impact on the safe operation of the plant. The report will still be 
    required to be submitted each year and does not affect any plant 
    equipment or requirements for maintaining plant equipment. The 
    safety analysis assumptions will still be maintained, thus no 
    question of safety exists. Therefore, this change does not involve a 
    significant reduction in a margin of safety.
        (f) [Change [64] identified in Attachments A and D [of the 
    February 1, 1999, submittal]:
        This change proposes to relax the requirement for submitting the 
    (now-named) Annual Radiological Environmental Operating Report from 
    the currently required date of May 1 to May 15 of each year. May 15 
    is now the industry standard date for submittal of such reports.
        [1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, because:]
        The proposed change does not affect the probability of an 
    accident. The submittal date of this report is not assumed to be an 
    initiator of any analyzed event. Also, the consequences of an 
    accident are not affected by the submittal date of this report. This 
    proposed change does not impact the assumptions of any design basis 
    accident. This change will not alter assumptions relative to the 
    mitigation of an accident or transient event. This change has no 
    impact on the safe operation of the plant. The report will still be 
    required to be submitted each year and does not affect any plant 
    equipment or requirements for maintaining plant equipment. The 
    submittal date of this report is not required for the mitigation of 
    any accident. Therefore, this change will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        [2. Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, because:]
        The proposed change will not create the possibility of an 
    accident. This change will not physically alter the plant (no new or 
    different type of equipment will be installed). The change in method 
    governing submittal of this report does not affect current safety 
    analysis assumptions. Therefore, this change will not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
        [3. Involve a significant reduction in a margin of safety, 
    because:]
        The margin of safety i[s] not reduced by allowing the report to 
    be submitted 14 days later. This proposed change has no effect on 
    the assumptions of the design basis accident. This change has no 
    impact on the safe operation of the plant. The report will still be 
    required to be submitted each year and does not affect any plant 
    equipment or requirements for maintaining plant equipment. The 
    safety analysis assumptions will still be maintained, thus no 
    question of safety exists. Therefore, this change does not involve a 
    significant reduction in a margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
    
        NRC Section Chief: James W. Clifford.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: April 20, 1999.
    
        Description of amendment request: The amendment request proposes 
    changes to the existing requirements associated with the unloading and 
    loading of fuel in the reactor vessel.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        VY has determined that the proposed change to reload the reactor 
    core in a spiral pattern beginning around a Source Range Monitor 
    (SRM) does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The design basis 
    accident associated with refueling is the Refueling Accident; i.e., 
    the accidental dropping of a fuel bundle onto the top of the core. 
    There is no assumption as to
    
    [[Page 27329]]
    
    the core loading pattern in the analysis of this accident. The 
    analyzed abnormal operational transients associated with refueling 
    are: (1) the Control Rod Removal Error During Refueling, and (2) the 
    Fuel Assembly Insertion Error During Refueling. There is no 
    assumption as to the core loading pattern in the analyses of these 
    transients. The Fuel Assembly Insertion Error During Refueling 
    transient involves mislocated and rotated fuel assembly loading 
    errors. However, a change in the approved core loading pattern has 
    no impact on the probability of mislocating or rotating a bundle 
    while following that pattern. Furthermore, the proposed change 
    implements a core loading pattern that provides improved flux 
    monitoring as compared to the pattern prescribed by the current 
    Technical Specifications. When loading the core in accordance with 
    the proposed change, the SRM indication will be indicative of the 
    true flux of the loaded fuel, as the creation of flux traps 
    (moderator filled cavities surrounded on all sides by fuel) is 
    precluded.
        The Technical Specification Bases are under the purview of 
    10CFR50.59. As such, subsequent changes made via 10CFR50.59 to the 
    information relocated to the Bases are not allowed to increase the 
    probability or consequences of an accident previously evaluated. 
    Therefore, relocating the details of the core loading pattern to the 
    Bases does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The SRMs and the core loading pattern are not initiators of any 
    accident previously evaluated. As such, the subject changes cannot 
    affect the probability of an accident previously evaluated. The core 
    loading pattern is not assumed in the mitigation of any accident. 
    Since the proposed change provides improved flux monitoring by the 
    SRMs, operators will have more accurate indication and SRM automatic 
    trip functions will actuate more accurately. As such, any event 
    mitigation function provided by the SRMs is enhanced by this change. 
    Therefore, the associated changes do not involve a significant 
    increase in the consequences of an accident previously evaluated.
        2. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        VY has determined that the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. VY proposes to change the core reloading and 
    offloading patterns to start and stop, respectively, at an SRM 
    versus the geometric center of the core as prescribed by current 
    Technical Specifications. This ensures that flux monitoring 
    instrumentation is always OPERABLE in the fueled region of the 
    vessel. There is no separation of the monitoring device from the 
    fuel by cavities of water as is the case with the pattern prescribed 
    by the current Technical Specifications. As such, flux monitoring is 
    enhanced during core reloading and offloading. This change is 
    conservative relative to the current requirements. Therefore, no new 
    categories or types of accidents are created.
        Additionally, the Technical Specification Bases are under the 
    purview of 10CFR50.59. As such, subsequent changes made via 
    10CFR50.59 to the information relocated to the Bases are not allowed 
    to create the possibility for an accident or malfunction of a 
    different type than any evaluated previously in the safety analysis 
    report. Therefore, relocating the details of the core loading 
    pattern to the Bases does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not involve a 
    significant reduction in a margin of safety.
        VY has determined that the proposed change does not involve a 
    significant reduction in a margin of safety. Loading around the 
    geometric center of the core as prescribed by the current Technical 
    Specifications results in cells of moderator separating the fuel 
    from the instrumentation monitoring its flux. This change requires 
    the flux monitoring instrumentation to be in the fueled region, and, 
    in so doing, provides for more accurate monitoring of core flux 
    during core reloading and offloading. As such, the operators will 
    have more accurate indication and SRM automatic trip functions will 
    actuate when the actual flux reaches the trip setpoints. This 
    corrects non-conservatisms that result from cells of moderator 
    separating the fuel from the instrumentation. Therefore, this change 
    will not result in a significant reduction in a margin of safety.
        Additionally, the details of the loading pattern are relocated 
    from the Technical Specifications to the Bases. Since any future 
    changes to the Bases will be evaluated per the requirements of 10 
    CFR 50.59, no reduction in a margin of safety will be allowed. 
    Therefore, relocating the core loading pattern details to the Bases 
    does not involve a significant reduction in a margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
    
        NRC Section Chief: James W. Clifford.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: April 7, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise the minimum critical power ratio (MCPR) limit in Technical 
    Specification (TS) 2.1.1.2, for the ATRIUM-9X and the SVEA-96 fuel for 
    one and two recirculation loop operation. The proposed amendment would 
    add a new reference in TS 5.6.5, ``Core Operating Limits Report.'' The 
    reference cites ANFB Critical Power Correlation Uncertainty for Limited 
    Data Sets, ANF1125(P)(A), Supplement 1, Appendix D, Siemens Power 
    Corporation-Nuclear Division, July 1998.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The probability of an evaluated accident is derived from the 
    probabilities of the individual precursors to that accident. The 
    consequences of an evaluated accident are determined by the 
    operability of plant systems designed to mitigate those 
    consequences. Limits have been established consistent with NRC 
    approved methods to ensure that fuel performance during normal, 
    transient, and accident conditions is acceptable. The proposed 
    Technical Specifications amendment uses conservatively established 
    SLMCPR [safety limit minimum critical power ratio] values for WNP-2 
    such that the fuel is protected during normal operation as well as 
    during plant transients or anticipated operational occurrences.
        The probability of an evaluated accident is not increased by the 
    use of the ATRIUM-9X MCPR safety limit of 1.10 (two loop operation) 
    or 1.11 (single loop operation). The ATRIUM-9X fuel was evaluated by 
    SPC (Reference 5) [Letter KVW:98:148 dated July 8, 1998, KV Walters, 
    (Siemens Power Corporation), to RA Vopalensky (Supply System), 
    ``MCPR Safety Limit Reanalysis for WNP-2 Cycle 11''] using the 
    additive constant uncertainty for ATRIUM-9X fuel of 0.0201 which is 
    contained in the NRC safety evaluation approval of Reference 4 [ANFB 
    Critical Power Correlation Uncertainty for Limited Data Sets, ANF-
    1125(P)(A), Supplement 1, Appendix D, Siemens Power Corporation--
    Nuclear Division, July 1998]. Based upon the NRC approved additive 
    constant of uncertainty of 0.0201, as documented in Reference 5, at 
    least 99.9% of the SPC ATRIUM-9X fuel rods would be expected to 
    avoid boiling transition with a SLMCPR of 1.10 during two loop 
    operation and 1.11 during single loop operation.
        The probability of an evaluated accident is not increased by the 
    use of the ABB SVEA-96 SLMCPRs of 1.10 (two loop operation) or 1.12 
    (single loop operation). NRC approved
    
    [[Page 27330]]
    
    methodology documented in CENPD-300-P-A, ``Reference Safety Report 
    for Boiling Water Reactor Reload Fuel'', July 1996 (Reference 3) was 
    used in deriving these ABB SVEA-96 SLMCPR values. The ABB evaluation 
    as a function of cycle exposure established that late in Cycle 15 
    conservative two loop and single loop SLMCPRs of 1.10 and 1.12, 
    respectively, can be used to represent the entire cycle.
        The SLMCPR changes do not require any physical plant 
    modifications, physically affect any plant component, or entail 
    changes in plant operation. Therefore, no individual precursors of 
    an accident are affected.
        Since the operability of plant systems designed to mitigate any 
    consequences of accidents have not changed, the consequences of an 
    accident previously evaluated are not expected to increase.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Creation of the possibility of a new or different kind of 
    accident would require the creation of one or more new precursors of 
    that accident. New accident precursors may be created by 
    modifications of the plant configuration, including changes in 
    allowable modes of operation. This Technical Specification submittal 
    does not involve any modifications of the plant configuration or 
    allowable modes of operation. This Technical Specification change 
    establishes SLMCPRs for SPC fuel based upon the NRC approved 
    additive constant of uncertainty of 0.0201, as documented in 
    Reference 5. At least 99.9% of the SPC ATRIUM-9X fuel rods would be 
    expected to avoid boiling transition with an SLMCPR of 1.10 during 
    two loop operation or 1.11 during single loop operation. 
    Additionally, the ABB SVEA-96 SLMCPRs of 1.10 (two loop operation) 
    or 1.12 (single loop operation) were derived using the NRC approved 
    methodology documented in CENPD-300-P-P, ``Reference Safety Report 
    for Boiling Water Reactor Reload Fuel'', July 1996 (Reference 3). 
    Therefore, no new precursors of an accident are created and no new 
    or different kinds of accidents are created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Implementation of SLMCPRs derived by proven analytical methods 
    provides a margin of safety by ensuring that less than 0.1% of the 
    rods are expected to be in boiling transition if the MCPR limit is 
    not violated. Because the fuel design safety criteria of more than 
    99.9% of the fuel rods avoiding transition boiling during normal 
    operation as well as anticipated operational occurrences is met, 
    there is not a significant reduction in the margin of safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
    
        Attorney for licensee: Perry D. Robinson, Esq., Winston & Strawn, 
    1400 L Street, NW, Washington, DC 20005-3502.
    
        NRC Project Director: Stuart Richards.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: April 20, 1999.
    
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3.4.11, ``RCS Pressure and 
    Temperature Limits,'' to update the curves that set forth the pressure 
    temperature limit lines. The curves provide the pressure temperature 
    limits for the operation of the reactor coolant system for heatup and 
    cooldown during inservice leak and hydrostatic testing, non-nuclear 
    heating and cooldown, and nuclear heating and cooldown.
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The pressure temperature shift is well within the operating 
    margins of plant equipment. Using the new non-nuclear and nuclear 
    heating and cooldown curves, higher temperature values for 
    corresponding pressures at temperatures which are closest to RT 
    NDT, further reduce the potential for brittle fracture.
        The proposed 32 EFPY [effective full power years] curves were 
    developed using methodology that is consistent with the guidance in 
    Regulatory Guide 1.99, Revision 2, Appendix G of the ASME Code and 
    Appendix G of 10 CFR part 50. This methodology is recognized by the 
    NRC and the industry as providing acceptable margin.
        Therefore, operation of WNP-2 in accordance with the proposed 
    amendment will not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change has no impact on the previously analyzed 
    accidents or transients. The proposed change does not introduce any 
    credible mechanisms for unacceptable radiation release nor does it 
    require physical modification to the plant. The 32 EFPY curves are 
    calculated using a published methodology that was discussed with the 
    NRC.
        The proposed change is also within any upper bound limit. The 
    only impact on plant operation is that the plant will be operated 
    with new pressure temperature limits derived from the proposed 
    alternative calculational methodology in place of the previously 
    approved model based on actual plant data.
        Therefore, the operation of WNP-2 in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The results of testing reflected 30 ft-lb shifts and changes in 
    uppershelf energy of the base plate and the weld material. However, 
    the results are well within the values predicted by Regulatory Guide 
    1.99, Revision 2. Furthermore, the adjusted reference temperature 
    values and the upper shelf energy of the reactor beltline materials 
    are expected to remain within the limits of 10 CFR part 50, Appendix 
    G, for at least 32 effective full power years of reactor operation.
        For the non-nuclear and nuclear heating and cooldown curves 
    (with a calculated through wall T), lower temperatures 
    which are closest to RTNDT, have an increased margin of 
    safety due to the higher required temperature values for a given 
    pressure than is required by current curve calculation methodology. 
    Thus additional margin to brittle fracture is achieved for non-
    nuclear and nuclear heating.
        Therefore, operation of WNP-2 in accordance with the proposed 
    amendment will not involve a significant reduction in the margin of 
    safety.
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
    
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
    
        Attorney for licensee: Perry D. Robinson, Esq., Winston & Strawn, 
    1400 L Street, NW., Washington, DC 20005-3502.
    
        NRC Project Director: Stuart Richards.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait
    
    [[Page 27331]]
    
    for this biweekly notice or because the action involved exigent 
    circumstances. They are repeated here because the biweekly notice lists 
    all amendments issued or proposed to be issued involving no significant 
    hazards consideration.
    
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. Lucie 
    Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of amendment request: December 31, 1997, as supplemented May 
    15, September 15, November 25, 1998 and January 28, 1999.
    
        Description of amendment request: Revise the St. Lucie, Unit 2, 
    Technical Specifications to increase the capacity of the spent fuel 
    storage pool, in part, by allowing a credit for a certain soluble boron 
    concentration in the spent fuel pool.
    
        Date of publication of individual notice in the Federal Register: 
    April 5, 1999 (64 FR 16502).
    
        Expiration date of individual notice: May 5, 1999.
    
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of application for amendments: April 19, 1999.
    
        Brief description of amendments: The amendments would revise 
    Technical Specification Section 3/4.8.1.2, ``Electrical Power Systems, 
    Shutdown,'' and its associated bases to provide a one-time extension of 
    the 18-month surveillance interval for specific surveillance 
    requirements for Units 1 and 2. This surveillance will be performed 
    prior to the first entry into Mode 4 subsequent to receipt of the 
    requested T/S amendment. In addition, for Unit 2 only, a minor 
    administrative change is included to delete a reference to T/S 4.0.8, 
    which is no longer applicable. For Unit 1 only, an editorial change is 
    made to add the word ``or'' to action statement 3.8.1.2.
    
        Date of publication of individual notice in Federal Register: April 
    29, 1999 (64 FR 23129).
    
        Expiration date of individual notice: June 1, 1999.
    
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of Georgia, 
    City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, Edwin I. Hatch 
    Nuclear Plant, Units 1 and 2, Appling County, Georgia
    
        Date of amendment request: April 6, 1999.
    
        Description of amendment request: The proposed amendments would 
    allow an increase of 168 fuel assemblies in the storage capacity of 
    Unit 1's Spent Fuel Pool and an increase of 88 fuel assemblies in the 
    storage capacity of Unit 2's Spent Fuel Pool.
    
        Date of publication of individual notice in Federal Register: May 
    4, 1999 (64 FR 23877).
    
        Expiration date of individual notice: June 3, 1999.
    
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
    
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
    
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
    
        For further details with respect to the action see: (1) The 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois; Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: December 29, 1998.
    
        Brief description of amendments: The amendments change Technical 
    Specification Tables 3.3.1-1 and 3.3.2-1 to revise the Allowable Values 
    for 12 functions of the Reactor Trip System and Engineered Safety 
    Features Actuation System.
    
        Date of issuance: April 23, 1999.
    
        Effective date: Immediately, to be implemented within 30 days.
    
        Amendment Nos.: 107, 107, 100 and 100.
    
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
    
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9186). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 23, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois; Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: October 30, 1998.
    
        Brief description of amendments: The amendments revised the 
    Technical Specification (TS) requirements for
    
    [[Page 27332]]
    
    spent fuel pool inadvertent draindown elevation.
    
        Date of issuance: May 3, 1999.
    
        Effective date: Immediately, to be implemented within 30 days.
    
        Amendment Nos.: 108, 108 101, and 101.
    
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
    
        Date of initial notice in Federal Register: December 16, 1998 (63 
    FR 69335). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 3, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 0481.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    
        Date of application of amendment: June 2, 1998, and as supplemented 
    by letters dated January 18 and March 9, 1999.
    
        Brief description of amendment: The amendment relocates 
    requirements related to seismic monitoring instrumentation from the 
    Technical Specifications to the Technical Requirements Manual.
    
        Date of issuance: April 28, 1999.
    
        Effective date: Immediately; and shall be implemented within 60 
    days of issuance.
    
        Amendment No.: 194.
    
        Facility Operating License No. DPR-61: The amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: September 23, 1998 (63 
    FR 50936). The January 18 and March 9, 1999, supplements contained 
    revised TS pages to account for TS changes issued by the NRC since the 
    original June 2, 1998, submittal, pages from the Updated Final Safety 
    Analysis Report and TRM, which were revised to support the June 2, 
    1998, request, and additional clarifications. The supplemental 
    information did not change the staff's initial proposed no significant 
    hazards consideration determination or expand the scope of the original 
    notice. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 28, 1999.
    
        No significant hazards consideration received: No
    
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, Connecticut 06457.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: August 21, 1996, as supplemented 
    May 2, 1997.
    
        Brief description of amendment: The amendment revised Section 3.3.G 
    (Hydrogen Recombiner System and Post-Accident Containment Venting 
    System), the basis for Section 3.3.G, and Section 4.4, Table 4.4-1 
    (Containment Isolation Valves). This change permits removal of the 
    existing flame-type hydrogen recombiners, its supporting equipment, and 
    replacement with passive autocatalytic recombiners.
    
        Date of issuance: April 27, 1999.
    
        Effective date: As of the date of issuance to be implemented within 
    30 days.
    
        Amendment No.: 200.
    
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: Janaury 29, 1997 (62 FR 
    4345). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 27, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Consumers Energy Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of application for amendment: September 3, 1997.
    
        Brief description of amendment: The amendment revises TS 3.14, 
    Control Room Ventilation, to be consistent with NUREG-1432, Standard 
    Technical Specifications, Combustion Engineering Plants.
    
        Date of issuance: May 6, 1999.
    
        Effective date: May 6, 1999.
    
        Amendment No.: 186.
    
        Facility Operating License No. DPR-20: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: March 24, 1999 (64 FR 
    14281). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 6, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423-3698.
    
        Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, 
    Oconee Nuclear Station, Units 1, 2, and 3, Oconee County, South 
    Carolina
    
        Date of application of amendments: March 1, 1999.
    
        Brief description of amendments: The amendments revised the 
    Technical Specifications by adding a Note to Improved Technical 
    Specification (ITS) 3.9, ``Refueling Operations,'' Subsection 3.9.3, 
    ``Containment Penetrations,'' Limiting Condition for Operation 3.9.3.b, 
    to state that the emergency air lock door is not required to be closed 
    when it is sealed with the temporary cover plate.
    
        Date of Issuance: April 28, 1999.
    
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days of issuance.
    
        Amendment Nos.: Unit 1-303; Unit 2-303; Unit 3-303.
    
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: 
    Amendments revised the Technical Specifications.
    
        Date of initial notice in Federal Register: 64 FR 14282 (March 24, 
    1999). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 28, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
    Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: March 1, 1999.
    
        Brief description of amendments: The amendments revised the 
    Technical Specifications by changing the number of required channels 
    shown in TS Table 3.3.8-1, ``Post Accident Monitoring Instrumentation'' 
    for the Reactor Coolant System Hot Leg Temperature function from ``2 
    per loop'' to ``2.''
    
        Date of Issuance: April 28, 1999.
    
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days of issuance.
    
        Amendment Nos.: Unit 1-304; Unit 2-304; Unit 3-304
    
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: 
    Amendments revised the Technical Specifications.
    
        Date of initial notice in Federal Register: March 24, 1999 (64 FR 
    14281). The Commission's related evaluation of
    
    [[Page 27333]]
    
    the amendments is contained in a Safety Evaluation dated April 28, 
    1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of application for amendment: April 30, 1998.
    
        Brief description of amendment: The amendment revises the single 
    largest post-accident load capable of being supplied by the diesel 
    generators and relocates this value to the Bases for Technical 
    Specification (TS) Surveillance 4.8.1.1.2.c.3. TS Surveillance 
    4.8.1.1.2.c.3 has been revised to refer to ``the single largest post-
    accident load'' rather than a specific numerical value for diesel 
    generator load reject testing. This change is consistent with the 
    guidance provided in NUREG-1432 , ``Improved Standard Technical 
    Specifications for Combustion Engineering Plants.''
    
        Date of issuance: April 21, 1999.
    
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
    
        Amendment No.: 204.
    
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: October 21, 1998 (63 FR 
    56241). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 21, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Entergy Mississippi, Inc., 
    Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, Claiborne 
    County, Mississippi
    
        Date of application for amendment: July 21, 1995.
    
        Brief description of amendment: The amendment extends the 
    expiration date of Operating License NPF-29 for Grand Gulf Nuclear 
    Station, Unit 1, from June 16, 2022, to November 1, 2024. The extended 
    date is 40 years from the date the full-power license was issued for 
    the plant on November 1, 1984.
    
        Date of issuance: April 26, 1999.
    
        Effective date: As of the date of issuance to be implemented within 
    30 days of issuance.
    
        Amendment No: 137.
    
        Facility Operating License No. NPF-29: Amendment revises Operating 
    License No. NPF-29.
    
        Date of initial notice in Federal Register: August 16, 1995 (60 FR 
    42605). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 26, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120.
    
    Entergy Gulf States, Inc., and Entergy Operations, Inc., Docket No. 50-
    458, River Bend Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: December 16, 1998.
    
        Brief description of amendment: The amendment changes Technical 
    Specification (TS) Section 2.1.1.2, ``Reactor Core [Safety Limits],'' 
    by revising the two recirculation loop Minimum Critical Power Ratio 
    (MCPR) limit from 1.13 to 1.12 and the single recirculation loop MCPR 
    limit from 1.14 to 1.13. The revised limits are required to address the 
    River Bend Cycle 9 core design and operation. The proposed TS changes 
    are scheduled to be implemented following refueling outage 8, currently 
    scheduled to begin in April 1999.
    
        Date of issuance: April 27, 1999.
    
        Effective date: As of the date of issuance to be implemented prior 
    to the startup following refueling outage 8.
    
        Amendment No.: 105.
    
        Facility Operating License No. NPF-47: The amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9190). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 27, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
    
    Entergy Gulf States, Inc., and Entergy Operations, Inc., Docket No. 50-
    458, River Bend Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: October 8, 1998, as supplemented April 
    15, 1999.
    
        Brief description of amendment: The amendment implements the 
    Boiling Water Reactor Owners Group Enhanced Option I-A for the reactor 
    stability long-term solution to the neutronic and thermal hydraulic 
    instability that is documented in NEDO-32339, Revision 1, ``Reactor 
    Stability Long-Term Solution, Enhanced Option I-A.''
    
        Date of issuance: May 5, 1999.
    
        Effective date: As of the date of issuance and shall be implemented 
    during refueling outage 8.
    
        Amendment No.: 106.
    
        Facility Operating License No. NPF-47: The amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: November 18, 1998 (63 
    FR 64112). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 5, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit 3, Citrus County, Florida
    
        Date of application for amendment: October 30, 1998, as 
    supplemented March 31, 1999.
    
        Brief description of amendment: The amendment proposed to revise 
    the Final Safety Analysis Report (FSAR) and associated Improved 
    Technical Specification (ITS) Bases to reflect changes in the 
    methodology for the B spent fuel pool criticality analysis. The 
    proposed change is necessary due to Boraflex degradation in the B spent 
    fuel pool storage racks.
    
        Date of issuance: April 27, 1999.
    
        Effective date: April 27, 1999.
    
        Amendment No.: 175.
    
        Facility Operating License No. DPR-72: Amendment approves changes 
    to the FSAR and ITS Bases.
    
        Date of initial notice in Federal Register: December 30, 1998 (63 
    FR 71966). The supplemental letter dated March 31, 1999, did not change 
    the original no significant hazards consideration determination.
    
    
    [[Page 27334]]
    
    
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 27, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit 3, Citrus County, Florida
    
        Date of application for amendment: January 27, 1999.
    
        Brief description of amendment: The change would allow a one-time 
    extension of approximately 2 months of the steam generator tube 
    inspection interval in order for the inspection to coincide with the 
    next planned refueling outage.
    
        Date of issuance: May 5, 1999.
    
        Effective date: May 5, 1999.
    
        Amendment No.: 176.
    
        Facility Operating License No. DPR-72: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: March 10, 1999 (64 FR 
    11962). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 5, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. Lucie 
    Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of application for amendment: December 31, 1997, as 
    supplemented May 15, 1998, September 15, 1998, November 25, 1998, and 
    January 25, 1998.
    
        Brief description of amendment: This change modified the St. Lucie 
    Unit 2 Technical Specifications to increase the capacity of the spent 
    fuel storage pool, in part, by allowing a credit for a certain soluble 
    boron concentration in the spent fuel pool.
    
        Date of Issuance: May 6, 1999.
    
        Effective Date: Upon issuance of license amendment package with 
    implementation by the end of the next scheduled refueling outage, 
    currently scheduled for April of 2000.
    
        Amendment No.: 101.
    
        Facility Operating License No. NPF-16: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: February 11, 1998 (63 
    FR 6985) and December 16, 1998 (63 FR 69340). Following the receipt of 
    the supplement dated November 25, 1998, and the staff's subsequent no 
    significant hazards consideration determination (63 FR 69340), the 
    supplement dated January 28, 1999, contained clarifying information 
    that did not change the no significant hazards consideration 
    determination. An additional notice was required, in accordance with 10 
    CFR 2.1107, due to an oversight (64 FR 16502, April 5, 1999). An 
    environmental assessment has been published in the Federal Register (64 
    FR 23133, April 29, 1999). In that assessment, the Commission 
    determined that the issuance of this amendment will not result in any 
    environmental impacts other than those evaluated in the Final 
    Environmental Statement.
    
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated May 6, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Indian River Community College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34981-5596.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: February 24, 1999.
    
        Brief description of amendments: The amendments changed Technical 
    Specification (TS) 3/4.7.4 to permit the option of monitoring the 
    ultimate heat sink temperature afer the intake cooling water (ICW) 
    pumps but before the component cooling water heat exchangers which is 
    considered to be equivalent to temperature monitoring before the ICW 
    pumps.
    
        Date of issuance: May 5, 1999.
    
        Effective date: May 5, 1999.
    
        Amendment Nos.: 200 and 194.
    
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the TS.
    
        Date of initial notice in Federal Register: March 24, 1999 (64 FR 
    14282). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 5, 1999.
    
        No significant hazards consideration comments received: No
    
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: July 14, 1998
    
        Brief description of amendment: The proposed amendment changed the 
    Technical Specifications to revise the liquid and gaseous release rate 
    limits to reflect revisions to 10 CFR Part 20, ``Standards for 
    Protection Against Radiation.''
    
        Date of issuance: May 3, 1999.
    
        Effective date: May 3, 1999, to be implemented within 30 days from 
    the date of issuance.
    
        Amendment No.: 163.
    
        Facility Operating License No. DPR-36: The amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: January 13, 1999 (64 FR 
    2249). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 3, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: September 30, 1997.
    
        Brief description of amendment: The proposed amendment revises 
    portions of Facility Operating License No. DPR-36 to delete License 
    Conditions 2.B.6.c, 2.B.6.e, 2.B.6.f, 2.b.6.g, 2.b.7(a), and 2.B.7(b) 
    which are no longer applicable due to the permanently shutdown and 
    defueled condition of the Maine Yankee Atomic Power Station. Orders 
    dated May 23, 1980, August 29, 1980, and September 19, 1980, are 
    rescinded due to their being superseded by the equipment qualification 
    rule (10 CFR 50.49).
    
        Date of issuance: May 5, 1999.
    
        Effective date: May 5, 1999, and shall be implemented within 30 
    days from the date of issuance.
    
        Amendment No.: 164.
    
        Facility Operating License No. DPR-36: The amendment revised the 
    Operating License.
    
        Date of initial notice in Federal Register: December 3, 1997 (62 FR 
    63978). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 5, 1999.
    
    
    [[Page 27335]]
    
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of application for amendments: January 14, 1998, as 
    supplemented by letters dated May 19, 1998, September 28, 1998, and 
    three letters dated February 5, 1999.
    
        Brief description of amendments: The amendments authorize revisions 
    to the licensing basis as described in the Final Safety Analysis Report 
    (FSAR) Update to incorporate the modification to the 230 kV offsite 
    power system.
    
        Date of issuance: April 29, 1999.
    
        Effective date: April 29, 1999, and shall be implemented in the 
    next periodic update to the FSAR Update in accordance with 10 CFR 
    50.71(e).
    
        Amendment Nos.: Unit 1-132; Unit 2-130.
    
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Final Safety Analysis Report Update.
    
        Date of initial notice in Federal Register: October 7, 1998 (63 FR 
    53952). The supplemental letters dated September 28, 1998, and the 
    three letters dated February 5, 1999, provided additional clarifying 
    information, did not expand the scope of the application as originally 
    noticed, and did not change the staff's original proposed no 
    significant hazards consideration determination.
    
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated April 29, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, Diablo 
    Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis Obispo County, 
    California
    
        Date of application for amendments: September 3, 1998, as 
    supplemented by letters dated January 22, 1999, February 5, 1999, and 
    March 17, 1999.
    
        Brief description of amendments: The amendments change the 
    Technical Specifications to revise TS 3/4.4.9.1 Figures for heatup and 
    cooldown to extend their applicability to 16 effective full power 
    years.
    
        Date of issuance: May 3, 1999.
    
        Effective date: May 3, 1999, to be implemented within 30 days from 
    the date of issuance.
    
        Amendment Nos.: Unit 1-133; Unit 2-131.
    
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
    
        Date of initial notice in Federal Register: December 16, 1998 (63 
    FR69345). The supplemental letters dated January 22, 1999, February 5, 
    1999, and March 17, 1999 provided additional clarifying information and 
    did not change the staff's initial no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 3, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: January 7, 1999.
    
        Brief description of amendment: The amendment allows loading and 
    handling of spent fuel transfer and storage casks in the Trojan fuel 
    building.
    
        Date of issuance: April 23, 1999.
    
        Effective date: April 23, 1999.
    
        Amendment No.: 199.
    
        Facility Operating License No. NPF-1: The amendment changes the 
    Operating License.
    
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9197). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 23, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: January 27, 1999.
    
        Brief description of amendment: This proposed amendment would allow 
    unloading of spent fuel transfer casks in the Trojan Fuel Building.
    
        Date of issuance: April 23, 1999.
    
        Effective date: April 23, 1999.
    
        Amendment No.: 200.
    
        Facility Operating License No. NPF-1: The amendment revises the 
    Operating License.
    
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9198). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 23, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    
        Date of application for amendment: February 12, 1997.
    
        Brief description of amendment: The amendment deletes the 
    Independent Spent Fuel Storage Installation area from the Permanently 
    Defueled Technical Specifications.
    
        Date of issuance: May 5, 1999.
    
        Effective date: May 5, 1999.
    
        Amendment No.: 201.
    
        Facility Operating License No. NPF-1: The amendment changes the 
    Permanently Defueled Technical Specifications.
    
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9196). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 5, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
    
    Public Service Electric & Gas Company, Docket No. 50-272, Salem Nuclear 
    Generating Station, Unit No. 1, Salem County, New Jersey
    
        Date of application for amendment: January 15, 1999, as 
    supplemented on March 31, 1999.
    
        Brief description of amendment: The amendment allows a one-time 
    extension of the Technical Specification (TS) surveillance interval to 
    the end of fuel Cycle 13 (IR13) for certain TS
    
    [[Page 27336]]
    
    surveillance requirements (SRs). Specifically, the amendment extends 
    the surveillance interval in (a) SR 4.3.2.1.3 for the instrumentation 
    response time and sequence testing of each engineered safety features 
    actuation system (ESFAS) function; (b) SRs 4.8.2.3.2.f and 4.8.2.5.2.d 
    for service testing of the 125-volt DC and the 28-volt DC distribution 
    system batteries, respectively; (c) SR 4.8.2.5.2.c.2 for verification 
    of the condition of the 125-volt DC battery connections; (d) SR 
    4.8.3.1.a.1.a and 4.8.3.1.a.1.b for channel calibration and integrated 
    system functional test for containment penetration conductor 
    protection; (e) SR 4.1.2.2.c for verification that each automatic valve 
    in the reactivity control system flow path actuates on a safety 
    injection (SI) test signal; (f) SRs 4.3.1.1.1,Table 4.3-1, 4.3.2.1.1, 
    Table 4.3-2, 4.3.3.5, Table 4.36, and 4.3.3.7, Table 4.3-11 for the 
    channel calibration of containment water level-wide range, the manual 
    solid-state protection system (SSPS) functional input check, and the 
    ESFAS manual initiation channel functional test; (g) SR 4.5.1.d for 
    verification that each accumulator isolation valve opens automatically 
    on an SI test signal; (h) SR 4.5.2.e.1 for verification that each 
    automatic valve in the ECCS flow path actuates on an SI test signal, 
    (i) SR 4.7.6.1.d.2 for verification that the control room emergency air 
    conditioning system automatically actuates in the pressurization mode 
    on an SI test signal or control room intake high radiation test signal; 
    (j) SR 4.7.10.b for verification that each automatic valve in the 
    chilled water loop actuates on an SI signal; and (k) SR 4.8.1.1.2.d.7 
    which requires a test to verify that each emergency diesel generator 
    operates for at least 24 hours. The SRs are to be completed during the 
    next refueling outage (1R13), prior to returning the unit to Mode 4 
    (hot shutdown) upon outage completion. The amendment also makes some 
    administrative and editorial changes on some of the pages that will be 
    affected by the above SR interval extensions.
    
        Date of issuance: May 4, 1999.
    
        Effective date: May 4, 1999.
    
        Amendment No.: 222.
    
        Facility Operating License No. DPR-70: This amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: February 10, 1999 (64 
    FR 6709). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 4, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: February 8, 1999.
    
        Brief description of amendments: The amendments revise Technical 
    Specification 4.5.3.2.b to allow the option of using closed and 
    disabled automatic valves to provide the necessary isolation function 
    when performing safety injection and charging pump testing in Modes 4, 
    5, and 6 (i.e., hot shutdown, cold shutdown, and refueling) for low 
    temperature overpressurization protection.
    
        Date of issuance: April 26, 1999.
    
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
    
        Amendment Nos.: 220 and 202.
    
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
    
        Date of initial notice in Federal Register: March 24, 1999 (64 FR 
    14284). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 26, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: March 26, 1998.
    
        Brief description of amendments: The amendments revise Technical 
    Specification 3/4.8.2.1, ``AC Distribution--Operating,'' to add 
    operability conditions and associated action statements for the 115-
    volt vital instrument bus (VIB) D and inverter. The amendments complete 
    the recommended action from NRC Generic Letter 91-11, Resolution of 
    Generic Issues 48, ``LCOs for Class 1E Vital Instrument Buses,'' and 
    49, ``Interlocks and LCOs for Class 1E Tie Breakers,'' pursuant to 10 
    CFR 50.54(f), dated July 18, 1991.
    
        Date of issuance: April 30, 1999.
    
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
    
        Amendment Nos.: 221 and 203.
    
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
    
        Date of initial notice in Federal Register: May 6, 1998 (63 FR 
    25117). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 30, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. Ginna 
    Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: March 1, 1999.
    
        Brief description of amendment: The amendment revises the Ginna 
    Station Improved Technical Specifications battery cell parameters limit 
    for specific gravity (Surveillance Requirement (SR) 3.8.6.3 and SR 
    3.8.6.6).
    
        Date of issuance: April 23, 1999.
    
        Effective date: April 23, 1999.
    
        Amendment No.: 74.
    
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: March 24, 1999 (64 FR 
    14284). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 23, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: January 15,1999 (TS 98-07).
    
        Brief description of amendments: The amendments change the 
    Technical specifications (TS) by adding a new action statement to TS 
    3.1.3.2, ``Position Indicating Systems--Operating,'' that eliminates 
    the need to enter TS 3.0.3 whenever two or more individual rod position 
    indications per bank may be inoperable. It also allows additional time 
    to determine the position of the non indicating rod(s).
    
        Date of issuance: May 4, 1999.
    
        Effective date: May 4, 1999.
    
        Amendment Nos.: 244 and 235.
    
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the TS.
    
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR
    
    [[Page 27337]]
    
    9201). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 4, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: November 3, 1998.
    
        Brief description of amendment: The amendment makes changes to the 
    Technical Specifications to more clearly describe the emergency core 
    cooling system actuation instrumentation for the low pressure coolant 
    injection and core spray systems.
    
        Date of Issuance: April 26, 1999.
    
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
    
        Amendment No.: 170.
    
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: February 10, 1999 (64 
    FR 6714). The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated April 26, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 50-
    339, North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of application for amendments: July 28, 1998.
    
        Brief description of amendments: The amendments revise the 
    Technical Specifications Section 4.6.2.2.1.b for Units 1 and 2 casing 
    cooling and outside recirculation spray pumps surveillance testing 
    criteria.
    
        Date of issuance: April 22, 1999.
    
        Effective date: April 22, 1999.
    
        Amendment Nos.: 219 and 200.
    
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
    
        Date of initial notice in Federal Register: September 9, 1998 (63 
    FR 48272). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 22, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of amendment request: October 23, 1998.
    
        Brief description of amendment: The amendment revises Technical 
    Specification 3/4.5.1, ``Emergency Core Cooling Systems--
    Accumulators,'' by increasing the allowed outage time with one 
    accumulator inoperable for reasons other than boron concentration 
    deficiencies from 1 hour to 24 hours. The corresponding Bases section 
    was also revised.
    
        Date of issuance: April 27, 1999.
    
        Effective date: April 27, 1999, to be implemented within 30 days 
    from the date of issuance.
    
        Amendment No.: 124.
    
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
    
        Date of initial notice in Federal Register: November 18, 1998 (63 
    FR 64127). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 27, 1999.
    
        No significant hazards consideration comments received: No.
    
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of no Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
    
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
    
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
    
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
    
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
    
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action.
    
    [[Page 27338]]
    
    Accordingly, the amendments have been issued and made effective as 
    indicated.
    
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
    
        For further details with respect to the action see: (1) The 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
    
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By June 18, 1999, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
    
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
    
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
    
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
    
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
    
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Southern California Edison Company, et al., Docket No. 50-361, San 
    Onofre Nuclear Generating Station, Unit No. 2, San Diego County, 
    California
    
        Date of application for amendment: April 24, 1999.
    
        Brief description of amendment: This one-time temporary amendment 
    allows the facility to be outside the licensing basis regarding remote 
    shutdown capability of the shutdown cooling system as described in the 
    Updated Safety Analysis Report, Section 5.4.7.1.2, during the period of 
    the repair. The amendment is effective for 7 days from the date of 
    issuance or until the repair of the check valves is completed, 
    whichever occurs first.
    
        Date of issuance: April 26, 1999.
    
        Effective date: April 26, 1999, and is effective for 7 days from 
    the date of issuance or until the check valves repair is completed, 
    whichever occurs first.
    
        Amendment No.: 152.
    
        Facility Operating License Nos. NPF-10: This amendment approved a 
    one-time change to the design basis as described in the Updated Safety 
    Analysis Report.
    
        Public comments requested as to proposed no significant hazards 
    consideration: No.
    
    
    [[Page 27339]]
    
    
        The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, consultation with the State of California, and 
    final no significant hazards consideration determination are contained 
    in a Safety Evaluation dated April 26, 1999.
    
        Attorney for Licensee: T.E. Qubre, Esquire, Southern California 
    Edison Company, P.O. Box 800, Rosemead, California 91770
    
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
        NRC Section Chief: Stephen Dembek.
    
        Dated at Rockville, Maryland, this 12th day of May 1999.
    
        For the Nuclear Regulatory Commission.
    John A. Zwolinski,
    Director, Division of Licensing Project Management, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 99-12494 Filed 5-18-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
05/19/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-12494
Dates:
Immediately, to be implemented within 30 days.
Pages:
27315-27339 (25 pages)
PDF File:
99-12494.pdf