X96-20522. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 100 (Wednesday, May 22, 1996)]
    [Notices]
    [Pages 25696-25720]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-20522]
    
    
    
    =======================================================================
    -----------------------------------------------------------------------
    
    UNITED STATES NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from April 27, 1996, through May 10, 1996. The 
    last biweekly notice was published on May 8, 1996 (61 FR 20842).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By June 21, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with
    
    [[Page 25697]]
    
    the applicant on a material issue of law or fact. Contentions shall be 
    limited to matters within the scope of the amendment under 
    consideration. The contention must be one which, if proven, would 
    entitle the petitioner to relief. A petitioner who fails to file such a 
    supplement which satisfies these requirements with respect to at least 
    one contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: April 5, 1996
        Description of amendments request: Pursuant to 10 CFR 50.80 and 
    50.90, the Baltimore Gas and Electric Company (BGE) hereby requests the 
    transfer and amendment of Operating License Nos. DPR-53 and DPR-69 for 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2.
        The proposed license transfers and amendments are requested as part 
    of the pending merger between BGE and Potomac Electric Power Company 
    into Constellation Energy Corporation. The proposed license transfers 
    would transfer authority to possess and operate Calvert Cliffs from BGE 
    to Constellation Energy Corporation. The proposed amendments would 
    change the licenses as well as the related Technical Specifications, to 
    reflect this transfer by submitting Constellation Energy Corporation in 
    place of BGE as the licensee for Calvert Cliffs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed amendment will change the name of the licensee 
    authorized to possess and operate Calvert Cliffs Nuclear Power Plant 
    from Baltimore Gas and Electric Company (BGE) to Constellation 
    Energy Corporation. This amendment request is necessary because of a 
    proposed merger of BGE and Potomac Electric Power Company into 
    Constellation Energy Corporation. As a result of the savings 
    achieved through a reduction in operating costs due to the merger, 
    Constellation Energy Corporation will have the financial resources 
    to possess and operate Calvert Cliffs.
        In addition, Constellation Energy Corporation personnel will be 
    technically qualified to operate the plant. Baltimore Gas and 
    Electric Company nuclear personnel have been named to management 
    positions in Constellation Energy Corporation, and will remain 
    responsible for Calvert Cliffs operation and maintenance. The 
    proposed amendment involves no changes in the training program or 
    operating organization for Calvert Cliffs.
        The proposed amendment does not require any physical change to 
    the facilities or substantive modifications to the Technical 
    Specifications or to procedures. The proposed change does not 
    increase the probability of an accident previously evaluated because 
    it does not affect any initiators in any previously evaluated 
    accidents. The proposed change does not increase the consequences of 
    an accident previously evaluated because it does not affect any of 
    the items on which the consequences depend.
        Therefore, the proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed amendment does not modify the plant's configuration 
    or operations. As a result, no new accident initiators are 
    introduced. Therefore, the proposed amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        This amendment request is necessary because of a proposed merger 
    of BGE and Potomac Electric Power Company into Constellation Energy 
    Corporation. As a result of the savings achieved through a reduction 
    in operating costs due to the merger, Constellation Energy 
    Corporation will have the financial resources to possess and operate 
    Calvert Cliffs. Also, Constellation Energy Corporation personnel 
    will be technically qualified to operate the plant. Baltimore Gas 
    and Electric Company nuclear personnel have been named to management 
    positions in Constellation Energy Corporation, and will remain 
    responsible for Calvert Cliffs' operation and maintenance. The 
    proposed amendment involves no changes in the training program or 
    operating organization for Calvert Cliffs. In addition, the proposed 
    amendment to substitute Constellation Energy Corporation for BGE 
    does not result in any changes to the physical design or operation 
    of the plant. Therefore, the proposed amendment does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    [[Page 25698]]
    
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Susan Frant Shankman, Acting
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: April 2, 1996
        Description of amendments request: The proposed amendments revise 
    the Brunswick Steam Electric Plant, Units 1 and 2, Technical 
    Specifications (TS) to allow uprate of the units to 105 percent of 
    rated thermal power.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        . May the proposed activity involve a significant increase in 
    the probability or consequences of an accident evaluated previously 
    in the Safety Analysis Report?
        The increase in power level, steam flow, feedwater flow and 
    associated instrument setpoint changes will not significantly 
    increase the probability or consequences of an accident previously 
    evaluated.
        The probability (frequency of occurrence) of Design Basis 
    Accidents occurring is not affected by the increase in power level, 
    as plant equipment will remain in compliance with the applicable 
    regulatory criteria (ASME Codes, IEEE Standards, NEMA Standards, 
    Regulatory Guide criteria, etc.). The physical plant changes 
    necessary to support power uprate include instrument setpoint 
    changes, indicating meter scale changes for the RWCU [reactor water 
    cleanup] System flow and Main Steam Flow indicators, Leak Detection, 
    Process Computer, ERFIS [emergency response facility information 
    system], and Feedwater System software changes, and SRV [safety/
    relief valve] setpoint changes. The setpoints were calculated in 
    accordance with the CP&L Setpoint Methodology. Utilizing this 
    methodology ensures scram setpoints (instrument settings that 
    initiate automatic plant shutdowns) will be established such that 
    there is no significant increase in scram frequency due to uprate. 
    No new challenges to safety related equipment will result from power 
    uprate.
        The changes in consequences of hypothetical accidents which 
    would occur from 102% of the uprated power (2609 MWt), compared to 
    those previously evaluated from [greater than or equal to] 102% of 
    the original power (2485 MWt), are not significant, because the 
    accident evaluations at uprated power will not result in exceeding 
    the NRC approved acceptance limits. The spectrum of hypothetical 
    accidents and transients has been investigated, and those accidents/
    transients currently evaluated in the UFSAR [Updated Final Safety 
    Analysis Report] were shown to meet the plant's current regulatory 
    criteria at uprated conditions (105%). In the area of core design, 
    for example, the fuel operating limits will still be met at the 
    uprated power level, and fuel reload analyses show plant transients 
    will still meet the criteria accepted by the NRC as specified in 
    NEDO-24011, ``GESTAR II.'' Challenges to fuel or ECCS [emergency 
    core cooling system] performance have been evaluated and shown to 
    meet the criteria of 10CFR50 Appendix K. Challenges to the 
    containment have been evaluated and still meet 10CFR50 Appendix A 
    Criterion 38, Long Term Cooling, and Criterion 50, Containment. 
    Bounding events involving radiological releases have been evaluated 
    and were shown to be well within the criteria of 10CFR100.
        2. May the proposed activity create the possibility of a new or 
    different kind of accident from any accident previously evaluated in 
    the Safety Analysis Report?
        The change in reactor thermal power will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Equipment that could be affected by power uprate has been 
    evaluated. No new operating mode, safety related equipment lineup, 
    accident scenario, or equipment failure mode was identified. The 
    full spectrum of accident considerations defined in the BNP 
    [Brunswick Nuclear Plant] UFSAR has been evaluated and no new or 
    different kind of accident has been identified. Uprate uses 
    developed technology and applies it within the capabilities of 
    existing plant equipment in accordance with existing regulatory 
    criteria including NRC approved codes, standards, and methods. 
    General Electric has designed BWRs [Boiling Water Reactors] of 
    higher power levels than the uprated power of any of the currently 
    uprated BWR/4 fleet and has not identified new power dependent 
    accidents.
        The changes to the Technical Specifications required to 
    implement power uprate make little change to the plant's 
    configuration. These changes fall into three major categories. The 
    first includes those changes resulting from power uprate parameter 
    changes. These parameter changes, such as the increase in vessel 
    pressure, temperature and piping system flows are minor in nature. 
    The evaluations have shown the plant is still within its design 
    capabilities when operating under these conditions. The changes 
    required as a result of power uprate will not affect the design 
    function(s) of currently installed equipment; therefore, there is no 
    possibility of a new or different kind of failure mode. The second 
    set of changes is a result of applying setpoint methodology to 
    calculate TS Allowable Values and Normal Trip Setpoints for 
    instruments that are directly affected by the parameter changes due 
    to power uprate. By using CP&L's methodology, the TS values were 
    calculated to ensure adequate margin exists between the analytical 
    limit and the TS Allowable Value. The third change include [sic] 
    setpoints that were reconstituted by the power uprate project. 
    Again, CP&L methodology was applied and the results show the 
    setpoints have moved to a more conservative value. This will reduce 
    the likelihood of spurious scrams and unnecessary challenges to 
    safety systems while ensuring initiation/actuation equipment 
    continues to function consistent with existing accident analyses.
        3. Does the proposed activity involve a significant reduction in 
    a margin of safety defined in the basis of any Operating License 
    Technical Specification?
        Power Uprate will not involve a significant reduction in a 
    margin of safety. The bounding events which had been analyzed in the 
    UFSAR were reevaluated to demonstrate that power uprate can be 
    implemented without exceeding any analyzed limit. Because the 
    applicable safety analysis criteria and limits are satisfied for 
    power uprate, the margin of safety associated with the safety limits 
    and other limits identified in the Technical Specifications will be 
    maintained.
        As discussed in Section 5 of GE Nuclear Energy's License Topical 
    Report NEDO-31984P ``Generic Evaluations of General Electric Boiling 
    Water Reactor Power Uprate,'' the safety margins prescribed by the 
    Code of Federal Regulations (CFR) have been maintained by meeting 
    the appropriate regulatory criteria. Similarly, the margins provided 
    by the application of the ASME design criteria have been maintained. 
    The Brunswick unique analysis NEDC-32466P ``Power Uprate Safety 
    Analysis Report for Brunswick Steam Electric Plant Units 1 and 2'' 
    discusses the effects of power uprate on safety margins for (1) fuel 
    thermal limits, (2) design basis accidents and the challenges for 
    fuel, containment and radiological releases, (3) transient analysis, 
    (4) non-LOCA radiological releases, and (5) environmental 
    consequences. These evaluations conclude that applicable safety 
    analysis criteria and limits are satisfied, and thus, the margins of 
    safety will be maintained.
        The changes to the Technical Specification instrumentation will 
    not involve a reduction in the margin of safety. The calculations 
    performed for power uprate have established an analytical limit and 
    calculated the TS Allowable Value and Nominal Trip Setpoint using 
    formal setpoint methodology. This ensures the instrumentation 
    functional requirements are met.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Eugene V. Imbro
    
    [[Page 25699]]
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: March 29, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to add an allowance to 
    complete a TS required surveillance within 24 hours of discovery of a 
    missed surveillance in accordance with the guidance of Generic Letter 
    (GL) 87-09, ``Sections 3.0 and 4.0 of the Standard Technical 
    Specifications (STS) on the Applicability of Limiting Conditions for 
    Operation and Surveillance Requirements.'' The wording specifying 
    intervals for testing has been changed to reflect wording consistent 
    the new STS. Typographical errors in the basis are also being 
    corrected.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    1. The proposed changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes clarify and incorporates [sic] NRC guidance 
    for application of extending or moving surveillance intervals by 
    plus or minus 25%, by elimination of restrictive surveillance 
    interval descriptions that conflict with NRC guidance, by allowing 
    for an additional 24 hours to perform missed surveillances, and by 
    providing a defined finite period for the term ``immediate'' for 
    Technical Specification (TS) and Inservice Inspection (ISI) 
    surveillances. The basis for extending or moving surveillances, as 
    stated in GL 89-14, ``Line-Item Improvements in Technical 
    Specifications - Removal of the 3.25 Limit on Extending Surveillance 
    Intervals,'' is to provide plants flexibility for scheduling the 
    performance of surveillances and to permit consideration of plant 
    operating conditions that may not be suitable for conducting a 
    surveillance at the specified time interval. Such operating 
    conditions include transient plant operation or ongoing surveillance 
    or maintenance activities. Extending surveillance intervals during 
    plant operation can result in a benefit to safety when a scheduled 
    surveillances [sic] is due at a time that is not suitable for 
    conducting the scheduled surveillance. NUREG-1431, ``Standard 
    Technical Specifications - Westinghouse Plants,'' states ``the 25% 
    extension does not significantly degrade the reliability that 
    results from performing the surveillance at its specified 
    frequency.'' This is based on the recognition that the most probable 
    result of any particular surveillance being performed is the 
    verification of conformance with the surveillance requirements. The 
    basis for the 24 hour delay period, as stated in the basis for 
    NUREG-1431, includes consideration of unit conditions, adequate 
    planning, availability of personnel, the time required to perform 
    the surveillance, the recognition that the most probable result of 
    any particular surveillance being performed is the verification of 
    conformance with the requirements.'' The basis for defining the term 
    ``immediate'' is to provide guidance to plant personnel for 
    conducting operability testing of the Steam Driven Auxiliary 
    Feedwater pump after extended shutdown periods in order to minimize 
    plant risks and not pose an unsafe operational transient during an 
    unstable plant configuration (i.e., during plant startup). Since 
    these changes do not affect plant design, operation, or the manner 
    in which testing is performed, the proposed changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes clarify and incorporates [sic] NRC guidance 
    for application of extending or moving surveillance intervals by 
    plus or minus 25%, by elimination of restrictive surveillance 
    interval descriptions that conflict with NRC guidance, by allowing 
    for an additional 24 hours to perform missed surveillances, and by 
    providing a defined finite period for the term ``immediate'' for TS 
    and ISI surveillances. Since these changes do not affect plant 
    design, operation, or the manner in which testing is performed, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety.
        The changes proposed, with the exception of allowing an 
    additional 24 hours to complete missed surveillances, are to clarify 
    existing surveillance intervals and to provide more specific and 
    detailed criteria without changing current surveillance scheduling 
    methodologies. The NRC has determined that allowing an additional 24 
    hours to complete missed surveillance tests minimizes additional 
    challenges to plant operations such that there is a conservative 
    balance between the risk associated with performing the surveillance 
    during stable plant conditions and the risk of imposing a plant 
    transient due to TS action statements or changing ``modes'' of 
    operation. These extensions are current industry practices endorsed 
    by the NRC which provide flexibility for scheduling and performing 
    surveillances and permit consideration of plant operating conditions 
    that may not be suitable for conducting a surveillance at either the 
    specified time interval or inadvertently missing the surveillance 
    interval. The risk to safety is low in contrast to the alternatives; 
    therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Eugene V. Imbro
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: April 8, 1996
        Description of amendment request: The proposed amendments would 
    change various sections of the Technical Specifications (TS) to reflect 
    the transition of fuel supplier from Generic Electric to Siemens Power 
    Corporation (SPC). The amendments would revise the definitions and 
    Limiting Conditions for Operation related to Linear Heat Generation 
    Rate, Critical Power Ratio, Maximum Critical Power Ratio, and Fraction 
    of Limiting Power Density to incorporate SPC terms and methodology or 
    to make the TS vendor neutral. Section 6.0 of the TS would be revised 
    to include SPC references. The proposed amendment also adds a 
    requirement to adjust the Average Planar Linear Heat Generation Rate 
    when the reactor is in single loop operation since SPC methodologies 
    may require this reduction factor for SPC fuel. The SPC methodologies 
    to be added to the TS have previously been approved by the NRC. The 
    proposed amendment would also relocate requirements for the traversing 
    in-core probe system from the TS to the Core Operating Limits Report 
    and would upgrade the fuel description in Section 5.0 as a line item 
    from the Improved Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    1. Involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The probability of an evaluated accident is derived from the 
    probabilities of the individual precursors to that accident. The 
    consequences of an evaluated accident are determined by the 
    operability of plant
    
    [[Page 25700]]
    
    systems designed to mitigate those consequences. Limits will be 
    established consistent with NRC approved methods to ensure that fuel 
    performance during normal, transient, and accident conditions is 
    acceptable. The proposed Technical Specifications amendment reflects 
    previously approved SPC methodology used to analyze normal 
    operations, including anticipated operational occurrences (AOOs), 
    and to determine the potential consequences of accidents.
        Licensing Methods and Models
        The proposed amendment is to support operation with NRC approved 
    fuel and licensing methods supplied from Siemens Power Corporation. 
    In accordance with FSAR Chapter 15, the same accidents and 
    transients will be analyzed with the new fuel and methods as were 
    analyzed by GE for GE fuel. The analysis methods and models are NRC 
    approved (Note the mixed core treatment of critical power ratio is 
    being addressed under separate correspondence). These approved 
    methods and models are used to determine the fuel thermal limits. 
    Traversing In-core Probe (TIP) uncertainty are assumptions in the 
    approved Siemens core monitoring methodologies. The SPC core 
    monitoring code enables the site to monitor keff as well as rod 
    density to perform the reactivity anomaly surveillance. This is 
    consistent with GE methodology. Therefore, the change in licensing 
    analysis methods and models does not significantly increase the 
    probability of an accident or the consequences of an accident 
    previously identified. The support systems for minimizing the 
    consequences of transients and accidents are not affected by the 
    proposed amendment.
        New Fuel Design
        The use of ATRIUM 9B fuel at LaSalle does not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated in the FSAR. The ATRIUM-9B fuel is 
    generically approved for use as a reload BWR fuel type. (See Boiling 
    Water Reactor Licensing Methodology Summary, Siemens Power 
    Corporation, EMF-94-217(NP)). Limiting postulated occurrences and 
    normal operation have been analyzed using NRC-approved methods for 
    the ATRIUM 9B fuel design to ensure that safety limits are protected 
    and that acceptable transient and accident performance is 
    maintained.
        The reload fuel has no adverse impact on the performance of in-
    core neutron flux instrumentation or control rod drive response. The 
    ATRIUM-9B fuel design will not adversely affect performance of 
    neutron instrumentation nor will it adversely affect the movement of 
    control blades. The exterior dimensions of the ATRIUM-9B fuel 
    assembly are essentially identical to the GE9B; the ATRIUM-9B fuel 
    assembly for LaSalle uses a standard fuel channel and normal control 
    cell positioning (i.e., no offset). Thus, no adverse interactions 
    with the adjacent control blade and nuclear instrumentation are 
    anticipated. Additionally, given the above mentioned overall 
    envelope similarities, no problems are anticipated with other 
    station equipment such as the fuel storage racks, the new fuel 
    inspection stand and the spent fuel pool fuel preparation machine.
        The ATRIUM 9B design is neutronically compatible with the 
    existing fuel types and core components in the LaSalle core. SPC 
    tests have demonstrated that the ATRIUM-9B fuel design is 
    hydraulically compatible with the GE9 fuel. The bundle pressure drop 
    characteristics of the ATRIUM 9B bundle are similar to those of the 
    GE9 fuel design, hence core thermal-hydraulic stability 
    characteristics are not adversely affected by the ATRIUM 9B design.
        An evaluation of the Emergency Procedures is being performed to 
    ensure that the use of the ATRIUM-9B fuel at LaSalle does not alter 
    any assumptions previously made in evaluating the radiological 
    consequences of an accident at LaSalle Station.
        Methods approved by the NRC are being used in the evaluation of 
    fuel performance during normal and abnormal operating conditions. 
    The ComEd and SPC methods to be used for the cycle specific 
    transient analyses have been previously NRC approved. The exception 
    is the mixed core treatment of critical power ratio, which is being 
    addressed under separate correspondence.
        The description of the fuel is expanded to be consistent with 
    NUREG-1434. The description of the fuel materials, lead test 
    assembly use, and stating that designs must have been analyzed with 
    NRC Staff approved codes does not change existing methods; it only 
    describes them.
        Review of the above concludes that the probability of occurrence 
    and the consequences of an accident previously evaluated in the 
    safety analysis report have not been significantly increased.
        * * * * *
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated:
        Creation of the possibility of a new or different kind of 
    accident would require the creation of one or more new precursors of 
    that accident. New accident precursors may be created by 
    modifications of the plant configuration, including changes in 
    allowable modes of operation.
        Licensing Methods and Models
        The proposed Technical Specification amendment reflects 
    previously approved SPC methodology used to analyze normal 
    operations, including AOOs, and to determine the potential 
    consequences of accidents. As stated above, the proposed changes do 
    not permit modes of reactor operation which differ from those 
    currently permitted.
        New Fuel Design
        The basic design concept of a 9x9 fuel pin array with an 
    internal water box has been used in various lead assembly programs 
    and in reload quantities in Europe since 1986. WNP-2 has loaded 
    reload quantities since 1991. Approximately 650 water box assemblies 
    have been irradiated in the United States through 1995, with a 
    substantially higher number being irradiated overseas. The NRC has 
    reviewed and approved the ATRIUM-9B fuel design. (See Boiling Water 
    Reactor Licensing Methodology Summary, Siemens Power Corporation, 
    EMF-94-217(NP)). The similarities in fuel design and operation 
    indicate there would be no expectation of introducing new or 
    different types of accidents than have been considered for the 
    existing fuel. Therefore, the use of ATRIUM-9B fuel at LaSalle does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        * * * * *
        3. Involve a significant reduction in the margin of safety for 
    the following reasons:
        The existing margin to safety is provided by the existing 
    acceptance criteria (e.g., 10CFR50.46 limits). The proposed 
    Technical Specification amendment reflects previously approved SPC 
    methodology used to demonstrate that the existing acceptance 
    criteria are satisfied. The revised methodology has been previously 
    reviewed and approved by the USNRC for application to reload cores 
    of GE BWRs. References for the Licensing Topical Reports which 
    document this methodology, and include the Safety Evaluation Reports 
    prepared by the USNRC, are added to the Reference section of the 
    Technical Specifications as part of this amendment.
        Licensing Methods and Models
        The proposed amendment does not involve changes to the existing 
    operability criteria. NRC approved methods and established limits 
    (implemented in the Core Operating Limits Report) ensure acceptable 
    margin is maintained. The ComEd and SPC reload methodologies for the 
    ATRIUM-9B reload design are consistent with the Technical 
    Specification Bases. The Limiting Conditions for Operation are taken 
    into consideration while performing the cycle specific and generic 
    reload safety analyses. NRC approved methods are listed in 
    Specification 6.0 of the Technical Specifications.
        Analyses performed with NRC-approved methodology have 
    demonstrated that fuel design and licensing criteria will be met 
    during normal and abnormal operating conditions. Therefore, there is 
    not a significant reduction in the margin of safety.
        New Fuel Design
        The exterior dimensions of the ATRIUM-9B fuel assembly are 
    essentially identical to the GE9B; the ATRIUM-9B fuel assembly for 
    LaSalle uses a standard fuel channel and normal control cell 
    positioning; i.e., no offset. Thus, no adverse interactions with the 
    adjacent control blade and nuclear instrumentation are anticipated. 
    The change does not adversely impact equipment important to safety 
    and, therefore does not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One
    
    [[Page 25701]]
    
    First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: April 9, 1996
        Description of amendment request: The proposed amendments would 
    eliminate the automatic reactor scram function and the group 1 and 3 
    isolation valve closure functions associated with the Main Steam Line 
    Radiation Monitoring (MSLRM) system high radiation setpoint. 
    Elimination of these functions will eliminate potential spurious scrams 
    and isolations caused by increased main steam line radiation levels 
    during hydrogen injection. The licensee also proposes to raise the 
    MSLRM system alarm setpoints which are not part of the Technical 
    Specifications to include increased background radiation during 
    hydrogen injection. The proposed amendment would also delete the 
    surveillance requirements for the associated instruments.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        Redefining the full power radiation background, thus changing 
    the MSLRM alarm setpoint, does not change the probability of 
    occurrence of any accident which has been postulated and analyzed in 
    the UFSAR, but will reduce the probability of the inadvertent MSIV 
    closure transient which is an analyzed transient in the UFSAR. It 
    does not change the probability of malfunction of any equipment 
    important to safety associated with [loss of coolant accident] LOCA, 
    fuel handling accident or [control rod drop accident] CRDA. It also 
    does not change the resultant offsite radiological dose from the 
    bounding design basis CRDA. This is based upon all radioactivity, 
    resulting from the design basis CRDA, going to the condenser 
    instantaneously (or independent of the actual MSLRM setpoint) in the 
    offsite dose calculation.
        The elimination of reactor scram and isolation of MSIVs, 
    isolation of main steam line drain valves and reactor water sample 
    line valves, associated with the MSLRM system actuation do not 
    introduce, mitigate, or reduce the probability of any design basis 
    accident, or any accident, evaluated in the UFSAR. The topical 
    report NEDO-31400A has shown that there is essentially no reasonable 
    radiological consequence benefit in a design basis CRDA of retaining 
    the MSLRM associated reactor scram and MSIV isolation function. In 
    addition, the probability of inadvertent scram and isolation is 
    reduced. The proposed change will not adversely impact the operation 
    of the [reactor protection system] RPS or [primary containment 
    isolation system] PCIS with respect to performing its other intended 
    safety functions. The proposed change will not affect the operation 
    of other plant systems or equipment important to safety. The 
    consequences of eliminating the automatic closure of the main steam 
    line drain isolation valves and reactor recirculation water sample 
    line isolation valves along with the MSIVs has been evaluated to be 
    negligible additions to the CRDA doses. A [LaSalle County Station] 
    LSCS unique analysis has demonstrated that the radiological doses as 
    a result of design basis CRDA are acceptable.
        The MSLRM system high radiation trip was intended to function in 
    response to a CRDA which has been previously evaluated. No credit 
    for MSIV closure was taken in the CRDA analysis since it postulates 
    that all the radioactive material assumed to be released from the 
    fuel is transported to the main condenser prior to MSIV closure. 
    Furthermore, the probability of a fuel failure is independent of the 
    operation of the MSLRM system.
        By eliminating the MSLRM induced MSIV closure, the Offgas system 
    can be utilized to reduce potential offsite doses after a CRDA. The 
    [mechanical vacuum pump] MVP is tripped no later than 15 minutes of 
    a Hi-Hi radiation alarm but analytically results in acceptable 
    offsite doses.
        Thus the proposed amendment will not increase the probability of 
    any accident previously evaluated, and the elimination of the MSLRM 
    isolation signal for MSIVs and other small containment valves will 
    not significantly increase the consequences of a CRDA as previously 
    evaluated.
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        Redefining the full power radiation background, thus changing 
    the actual MSLRM alarm setpoint, does not alter the configuration of 
    the plant. It does not revise any logic or function of the MSLRM 
    trip channels or add, replace, or delete any equipment important to 
    safety. Therefore it does not introduce any new failure modes or 
    create any possibility of a new accident which may challenge safety 
    to the public and has not been previously analyzed. It also does not 
    involve any equipment which either has not been evaluated 
    previously, or may have any safety consequences to the public.
        The proposed Technical Specification changes involve eliminating 
    the MSLRM system high radiation trip function for initiating an 
    automatic reactor scram, and automatic isolations. The proposed 
    changes will not affect the operation of other plant systems or 
    equipment important to safety. The MSLRM system will continue to 
    initiate alarms as before. Plant procedures will be in place to take 
    appropriate mitigative measures in response to a high alarm.
        The isolation and reactor scram functions associated with the 
    MSLRM system actuation were originally intended to mitigate, not 
    prevent, a potential accident scenario such as a CRDA or gross fuel 
    failure event. Adding or removing an electronic signal, such as the 
    one from the MSLRM system, does not change system or hardware design 
    within the reactor vessel pressure boundary, and therefore will not 
    create the possibility of a new or different kind of accident from 
    those evaluated in the UFSAR like a LOCA or CRDA during power 
    operation. It also does not create the possibility of a new or 
    different kind of accident outside the reactor vessel pressure 
    boundary from those evaluated in the UFSAR, such as a LOCA or Fuel 
    Handling Accident. Removing the isolation signal also reduces the 
    probability of inadvertent scram and isolation.
        Therefore the proposed amendment will not create the possibility 
    of a new or different kind of accident from any accident previously 
    analyzed.
        3) Involve a significant reduction in the margin of safety 
    because:
        The current MSLRM trip Hi-Hi alarm setpoint (about 4 R/hour with 
    full power background at 1.3 R/hour) is at 3 times the full power 
    radiation background. As indicated in the plant unique analytical 
    result for LSCS, the radiological reading at the MSLRMs for design 
    basis CRDA is equivalent to over 1200 times the normal full power 
    radiation background (1600 R/hour divided by 1.3 R/hour), or 150 
    times the full power radiation background during peak HWC 
    environment (since the radiation background is 8 times the normal 
    background). Thus the safety margin was very large, and would still 
    be quite large with the HWC background factored into the MSLRM 
    actuation setpoint (3 x 8 x 1.3 = about 50). The Hi alarm setpoint 
    of 1.5 times full power background likewise will have a higher 
    safety margin. Thus there is basically no adverse consequence to the 
    margin of safety in the basis for the LaSalle technical 
    specifications.
        The proposed Technical Specification changes to eliminate the 
    MSLRM system high radiation trip function for initiating an 
    automatic reactor scram, and automatic closure of the MSIVs, main 
    steam line drain isolation valves, and reactor recirculation water 
    sample line isolation valves do not cause radiological dose 
    consequences to exceed the limit established by SRP 15.4.9.
        Per NEDO-31400A, the elimination of MSLRM trip/scram signal will 
    result in the reduction of potential inadvertent scrams, unnecessary 
    safety-related actuations, undue vessel isolation, and duty 
    challenges during normal plant operation. These can be interpreted 
    to be a potential reduction in core damage frequency, which 
    translates to an improvement in the margin of safety.
        Thus the margin of safety as defined in the basis of the 
    technical specifications is essentially unaffected, and is therefore 
    acceptable.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the
    
    [[Page 25702]]
    
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: April 16, 1996
        Description of amendment request: The proposed amendments would 
    eliminate the Technical Specification requirement to perform response 
    time testing for selected instruments. The instruments affected are the 
    sensors for selected reactor protection system instrumentation, main 
    steam isolation actuation instrumentation, and all sensors for 
    emergency core cooling system (ECCS) actuation instrumentation. The 
    proposed changes are supported by analyses performed by the Boiling 
    Water Reactor Owners' Group as documented in NEDO-32291-A which was 
    approved by the NRC for use in license amendment applications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    1) Involve a significant increase in the probability or consequences of 
    an accident previously evaluated because:
        The purpose of the proposed Technical Specification (TS) change 
    is to eliminate response time testing requirements for selected 
    components in the Reactor Protection System (RPS), Isolation 
    Actuation instrumentation and Emergency Core Cooling System (ECCS) 
    actuation instrumentation. The Boiling Water Reactor Owners' Group 
    (BWROG) has completed an evaluation which demonstrates that response 
    time testing is redundant to the other TS-required testing. These 
    other tests, in conjunction with actions taken in response to NRC 
    Bulletin 90-01, ``Loss of Fill-Oil in Transmitters Manufactured by 
    Rosemount,'' and Supplement 1, are sufficient to identify failure 
    modes or degradations in instrument response time and ensure 
    operation of the associated systems within acceptable limits. There 
    are no known failure modes that can be detected by response time 
    testing that cannot also be detected by the other TS-required 
    testing. This evaluation was documented in NEDO-32291-A, ``System 
    Analyses for the Elimination of Selected Response Time Testing 
    Requirements,'' dated October 1995. LaSalle County Station, LaSalle, 
    has confirmed the applicability of this evaluation to LaSalle. In 
    addition, LaSalle will complete the actions identified in the NRC 
    staffs safety evaluation of NEDO-32291-A.
        Because of the continued application of other existing TS-
    required tests such as channel calibrations, channel checks, channel 
    functional tests, and logic system functional tests, the response 
    time of these systems will be maintained within the acceptance 
    limits assumed in plant safety analyses and required for successful 
    mitigation of an initiating event. The proposed changes do not 
    affect the capability of the associated systems to perform their 
    intended function within their required response time, nor do the 
    proposed changes themselves affect the operation of any equipment. 
    As a result, LaSalle has concluded that the proposed changes do not 
    involve a significant increase in the probability or the 
    consequences of an accident previously evaluated.
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        The proposed changes only apply to the testing requirements for 
    the components identified above and do not result in any physical 
    change to these or other components or their operation. As a result 
    no new failure modes are introduced. Therefore, the proposed changes 
    do not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3) Involve a significant reduction in the margin of safety 
    because:
        The current TS-required response times are based on the maximum 
    allowable values assumed in the plant safety analyses. These 
    analyses conservatively establish the margin of safety. As described 
    above, the proposed changes do not affect the capability of the 
    associated systems to perform their intended function within the 
    allowed response time used as the basis for the plant safety 
    analyses. The potential failure modes for the components within the 
    scope of this request were evaluated for impact on instrument 
    response time. This evaluation confirmed that, with the exception of 
    loss of fill-oil of Rosemount transmitters, the remaining TS-
    required testing is sufficient to identify failure modes or 
    degradations in instrument response times and ensure that operation 
    of the applicable instrumentation is within acceptable limits. The 
    actions taken in response to NRC Bulletin 90-01 and Supplement 1 are 
    adequate to identify loss of fill-oil failures of Rosemount 
    transmitters. As a result, it has been concluded that plant and 
    system response to an initiating event will remain in compliance 
    with the assumptions of the safety analysis.
        Further, although not explicitly evaluated, the proposed changes 
    will provide an improvement to plant safety and operation by the 
    following:
        a. Reducing the time safety systems are unavailable,
        b. Reducing the potential for safety system actuations,
        c. Reducing plant shutdown risk,
        d. Limiting radiation exposure to plant personnel, and
        e. Eliminating the diversion of key personnel resources to 
    conduct unnecessary testing.
        Therefore, LaSalle has concluded that this request will not 
    significantly reduce the margin of safety, and may actually cause an 
    increase in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: November 2, 1994
        Description of amendment request: The proposed amendments would 
    delete the content of Appendix B, ``Environmental Protection Plan'' 
    (nonradiological), and modify License Condition 2.C.(2) to delete that 
    portion which refers to the Environmental Protection Plan.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [The proposed amendments would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated]:
        Deletion of the Environmental Protection Plan and modifying 
    License Condition 2.C.(2) will have no impact on the probability or 
    consequences of an accident previously evaluated because the changes 
    will not have any impact upon the design or operation of any plant 
    systems or components.
        2. [The proposed amendments would not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated]:
        The proposed revision will not create the possibility of a new 
    or different kind of accident from any previously evaluated because 
    the revision is administrative in nature and will not change the 
    types and amounts of effluent that will be released.
        3. [The proposed amendments would not involve a significant 
    reduction in a margin of safety]:
    
    [[Page 25703]]
    
        The proposed revision will not reduce a margin of safety because 
    it is administrative in nature and will not [a]ffect the margin of 
    safety as defined in the basis for any Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    Power Station, Unit 2, Shippingport, Pennsylvania
    
        Date of amendment request: April 29, 1996
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 5.3.1 to allow the use of ZIRCO as 
    an alternate zirconium-based fuel rod material and remove the word clad 
    since it has been eliminated from the text of the NRC's improved 
    Standard Technical Specifications (NUREG-1431). Limited substitution of 
    fuel rods by ZIRCO filler rods would also be permitted. The proposed 
    amendment would revise Note 2 on TS Table 3.9-1 to specify that the 
    maximum burnup in the peak fuel rod in a fuel assembly stored in Region 
    2 spent fuel racks should not exceed the NRC-approved limit for WCAP-
    12610 rather than the current maximum burnup limit of 60 GWD/MTU.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The methodologies used in the accident analyses remain 
    unchanged. The proposed changes do not change or alter the design 
    assumptions for the systems or components used to mitigate the 
    consequences of an accident. Use of ZIRLO fuel rod material does not 
    adversely affect fuel performance or impact nuclear design 
    methodology. Therefore, accident analysis results are not impacted.
        The operating limits will not be changed and the analysis 
    methods to demonstrate operation within the limits will remain in 
    accordance with NRC approved methodologies. Other than the changes 
    to the fuel assemblies, there are no physical changes to the plant 
    associated with this technical specification change. A safety 
    analysis will continue to be performed for each cycle to demonstrate 
    compliance with all fuel safety design bases.
        VANTAGE 5 fuel assemblies with ZIRLO fuel rods meet the same 
    fuel assembly and fuel rod design bases as other VANTAGE 5 fuel 
    assemblies. In addition, the 10 CFR 50.46 criteria are applied to 
    the ZIRLO fuel rods. The use of these fuel assemblies will not 
    result in a change to the reload design and safety analysis limits. 
    Since the original design criteria are met, the ZIRLO fuel rods will 
    not be an initiator for any new accident. The fuel rod material is 
    similar in chemical composition and has similar physical and 
    mechanical properties as Zircaloy-4. Thus, the fuel rod integrity is 
    maintained and the structural integrity of the fuel assembly is not 
    affected. ZIRLO improves corrosion performance and dimensional 
    stability. No concerns have been identified with respect to the use 
    of an assembly containing a combination of Zircaloy-4 and ZIRLO fuel 
    rods.
        The dose predictions in the safety analyses are not sensitive to 
    the fuel rod material used; therefore, the radiological consequences 
    of accidents previously evaluated in the safety analysis remain 
    valid. A reload analysis is completed for each cycle, in accordance 
    with NRC approved methodologies. Therefore, the proposed change does 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        VANTAGE 5 fuel assemblies with ZIRLO fuel rods satisfy the same 
    design bases as those used for other VANTAGE 5 fuel assemblies. All 
    design and performance criteria continue to be met and no new 
    failure mechanisms have been identified. The ZIRLO fuel rod material 
    offers improved corrosion resistance and structural integrity.
        The proposed changes do not affect the design or operation of 
    any system or component in the plant. The safety functions of the 
    related structures, systems, or components are not changed in any 
    manner, nor is the reliability of any structure, system, or 
    component reduced. The changes do not affect the manner by which the 
    facility is operated and do not change any facility design feature, 
    structure, or system. No new or different type of equipment will be 
    installed. Since there is no change to the facility or operating 
    procedures, and the safety functions and reliability of structures, 
    systems, or components are not affected, the proposed changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The use of Zircaloy-4, ZIRLO, or stainless steal filler rods in 
    fuel assemblies will not involve a significant reduction in the 
    margin of safety because analyses using NRC approved methodology 
    will be performed for each configuration to demonstrate continued 
    operation within the limits that assure acceptable plant response to 
    accidents and transients. These analyses will be performed using NRC 
    approved methods that have been approved for application to the fuel 
    configuration.
        Use of ZIRLO as fuel rod material does not change the VANTAGE 5 
    reload design and safety analysis limits. The use of these fuel 
    assemblies will take into consideration the normal core operating 
    conditions allowed in the technical specifications. For each reload 
    core, the fuel assemblies will be evaluated using NRC approved 
    reload design methods, including consideration of the core physics 
    analysis peaking factors and core average linear heat rate effects.
        Based on the above, it is concluded that the proposed license 
    amendment request does not result in a significant reduction in 
    margin with respect to plant safety as defined in the UFSAR [Updated 
    Final Safety Analysis Report] or any plant technical specification 
    BASES.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 1500l.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Entergy Operations, Inc., Docket Nos. 50-313 and 50-368, Arkansas 
    Nuclear One, Unit Nos. 1 and 2 (ANO-1&2), Pope County, Arkansas
    
        Date of amendment request: May 2, 1996
        Description of amendment request: The proposed technical 
    specification amendments would extend the allowed outage times for 
    emergency diesel generators at Arkansas Nuclear One, Units 1 and 2 to 7 
    days with an additional, once per refueling cycle extension of 7 more 
    days for each machine.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The emergency diesel generators (EDGs) are backup alternating 
    current power sources
    
    [[Page 25704]]
    
    designed to power essential safety systems in the event of a loss of 
    offsite power. The EDGs are not accident initiators in any accident 
    previously evaluated. Probabilistic Safety Analysis (PSA) methods 
    were utilized in order to fully evaluate the EDG allowed outage time 
    (AOT) extension proposed in this submittal. The results of these 
    analyses indicate there is not a significant increase in the 
    probability of an accident previously evaluated. Therefore, this 
    change does not involve an increase in the probability of an 
    accident previously evaluated.
        The EDGs provide backup power to components that mitigate the 
    consequences of accidents. The current TSs allow for an EDG to be 
    removed from service for an AOT. The proposed amendment extends the 
    current AOT for an EDG. The proposed change does not allow any more 
    equipment to be removed from service at one time. The proposed 
    changes to the AOTs do not affect any of the assumptions used in 
    deterministic safety analysis. By extending the EDG AOT, the 
    consequences of an accident previously evaluated will remain 
    unchanged.
        The proposed change removes redundant requirements associated 
    with an inoperable emergency power supply from the TS for the 
    pressurizer proportional heaters. The operability requirements for 
    emergency power supplies and actions to be taken if an EDG is 
    inoperable are already addressed in the ANO-2 TS 3.8.1.1.
        The associated changes that remove the requirements to test the 
    EDGs if one or both offsite power supplies are inoperable, for an 
    inoperable station battery, for an inoperable component in the two 
    ESF electrical distribution systems, the accelerated testing 
    requirements of the EDGs, and the daily testing requirements for the 
    operable EDGs improve the reliability for the operable EDGs by 
    reducing the number of unnecessary starts and stops. By improving 
    the EDG reliability, this change will not increase the consequences 
    of the accidents previously evaluated.
        The other changes in this submittal associated with the bases 
    are considered administrative in nature and have no effect on the 
    consequences of an accident previously evaluated.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        This proposed change does not alter the design, configuration, 
    or method of operation of the plant. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The proposed changes do not affect the Technical Specification 
    limiting conditions for operation or their bases which support the 
    deterministic analyses used to establish the margin of safety.
        Calculations performed to analyze the change in risk based on 
    these changes produced acceptable values which are included in the 
    tables located in the description of changes section. These 
    calculated changes in risk fall well within that which is normally 
    considered acceptable. When the additional benefit of maintaining 
    the Emergency Diesel Generators available during shutdown cooling 
    operations associated with refueling outages in considered, the 
    overall change in risk is further reduced.
        The remaining proposed changes are either associated with 
    increasing EDG reliability or considered administrative in nature.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: November 20, 1995, as supplemented by 
    the letter dated December 15, 1995.
        Description of amendment request: The licensee has proposed to 
    revise the Grand Gulf Nuclear Station (GGNS), Unit 1, Technical 
    Specifications (TSs) as follows for the drywell, the drywell airlock, 
    and the drywell isolation valves:
        1. For the drywell in Limiting Condition of Operation (LCO) 
    3.6.5.1, the surveillance frequency interval for the drywell bypass 
    test in Surveillance Requirement (SR) 3.6.5.1.1 would be increased from 
    18 months to 10 years. For this interval change, an increased testing 
    frequency would be required if bypass performance degrades (i.e., the 
    leakage is greater than the limit for two consecutive tests) and the 
    application of SR 3.0.2, the allowance to extend the surveillance 
    interval by 25 percent, would be restricted to 12 months on the 10-year 
    interval. This includes deleting the Note in SR 3.6.5.1.1.
        2. For the drywell airlock in LCO 3.6.5.2, the following changes 
    are requested: (a) the leak rate SR 3.6.5.2.2 would be transferred from 
    the airlock LCO (3.6.5.2) to SR 3.6.5.1.3 in the drywell LCO (3.6.5.1), 
    (b) the requirement in SR 3.6.5.2.2 for the air lock to meet a specific 
    overall leakage limit would be deleted, (c) the Note in SR 3.6.5.2.2 
    that stated that an inoperable air lock door does not invalidate the 
    previous air lock leakage test would be deleted, (d) the test pressure 
    for the air lock leakage test in SR 3.6.5.2.2 would be reduced from 
    11.5 psig to 3 psid, and (e) the surveillance frequency interval for 
    the air lock leakage and interlock testing, required in SRs 3.6.5.2.1 
    and 3.6.5.2.2, would be increased from 18 months to 24 months.
        3. For the drywell airlock in LCO 3.6.5.2 and the drywell isolation 
    valves in LCO 3.6.5.3, the Action Notes, which identify that the 
    actions required by drywell LCO 3.6.5.1 must be taken when the drywell 
    bypass leakage limit is not met, would be deleted. Action C.1 of LCO 
    3.6.5.2 and its associated completion time would also be deleted.There 
    would also be changes to the Bases of the TSs for the above LCOs and 
    SRs, based on the proposed changes.
        Basis for proposed no significant hazards consideration 
    determination: The amendment request dated November 20, 1995, applied 
    to both the Grand Gulf Nuclear Station (GGNS) and the River Bend 
    Station (RSB); however, not all of the proposed amendments apply to 
    GGNS. This Notice only discusses the amendment request for GGNS. The 
    reference below to proposed amendments which do not apply to GGNS are 
    marked by ``[....]''.
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration in its 
    application dated November 20, 1995, which is presented below:
        Entergy Operations, Inc. proposes to change the current Grand 
    Gulf Nuclear Station (GGNS) [....] Technical Specifications. The 
    specific proposed changes are:
        1. The Surveillance Frequency [interval] for the drywell bypass 
    test is changed [increased] from 18 months to 10 years with an 
    increased testing frequency required if performance degrades.
        2. The following changes are requested for the drywell air lock 
    testing: (a) the leakage rate surveillance is moved from the air 
    lock Limiting Condition for Operation (LCO) to the drywell LCO, (b) 
    the requirement for the air lock to meet a specific overall leakage 
    limit is deleted, (c) the Note that an inoperable air lock door does 
    not invalidate the previous air lock leakage test is deleted, (d) 
    the GGNS test pressure for the air lock leakage test is changed 
    [reduced] from 11.5 psig to 3 psid, [...,] and ([e]) the 
    Surveillance Frequency [interval] for the air lock leakage test and 
    interlock test is changed [increased] from 18 months to 24 months.
        3. The Actions Notes in the drywell air lock LCO and the drywell 
    isolation valve LCO that identifies that the Actions required
    
    [[Page 25705]]
    
    by the drywell LCO must be taken when the drywell bypass leakage 
    limit is not met is deleted. [Action C.1 of LCO 3.6.5.2 and its 
    associated completion time would also be deleted.]
        [4. ...]
        The Commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 10 CFR 
    50.92(c). The proposed changes involve the withdrawal of operating 
    restrictions previously imposed because acceptable operation of the 
    Mark III primary containment design had not been demonstrated at the 
    time of licensing. As published in the Federal Register regarding no 
    significant hazards consideration criteria, granting of a relief, 
    based upon demonstration of acceptable operation from an operating 
    restriction that was imposed because acceptable operation had not 
    yet been demonstrated does not involve a significant hazards 
    consideration (Ref. 48 FR 14870). Furthermore, a proposed amendment 
    to an operating license involves no significant hazards 
    consideration if operation of the facility in accordance with the 
    proposed amendment would not: (1) involve a significant increase in 
    the probability or consequences of an accident previously evaluated; 
    or (2) create the possibility of a new or different kind of accident 
    from any accident previously evaluated; or (3) involve a significant 
    reduction in a margin of safety.
        Entergy Operations, Inc. has evaluated the no significant 
    hazards consideration in its request for this license amendment, 
    even though the above-mentioned criterion is satisfied by this 
    proposal. In accordance with 10 CFR 50.91(a), Entergy Operations, 
    Inc. is providing the analysis of the proposed amendment against the 
    three standards in 10 CFR 50.92(c). A description of the no 
    significant hazards consideration determination follows:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The requested changes are either administrative changes which 
    clarify the format of the requirement or change the requirement to 
    match the design bases of the plant, a change which relocates the 
    requirement to the Technical Specification Bases, or a change in 
    [the] surveillance interval. Each of these types of change are 
    discussed below:
        1. The administrative changes clarify the format of the 
    requirement or change the requirement to match the design bases of 
    the plant. Clarifying [the] administrative format of the Technical 
    Specifications does not result in any changes to the Technical 
    Specification requirements and, as a result, does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated. Also, changing the requirements of 
    the Technical Specifications to more closely match the design bases 
    of the plant will continue to assure that the plant will respond as 
    assumed in the accident analyses and, as a result, does not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed changes relocate information to the Technical 
    Specification Bases. In the Technical Specifications Bases the 
    relocated information will be maintained in accordance with 10 CFR 
    50.59 and subject to the change control provisions in Chapter 5 of 
    Technical Specifications. Since any changes to the Technical 
    Specifications Bases will be evaluated per the requirements of 10 
    CFR 50.59, no increase (significant or insignificant) in the 
    probability or consequences of an accident previously evaluated will 
    be allowed. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        3. The proposed changes in frequency for the drywell bypass 
    leakage and drywell air lock surveillances will continue to ensure 
    that no paths exist through passive drywell boundary components that 
    would permit gross leakage from the drywell to the primary 
    containment air space and result in bypassing the primary 
    containment pressure-suppression feature beyond the design basis 
    limit. The Mark III primary containment system satisfies General 
    Design Criterion 16 of Appendix A to 10 CFR Part 50. Maximum drywell 
    bypass leakage was determined previously by reviewing the full range 
    of postulated primary system break sizes. The limiting case was a 
    primary system small break loss of coolant accident (LOCA) and 
    yielded a design allowable drywell bypass leakage rate limit of 
    approximately 35,000 scfm for GGNS [....]. The Technical 
    Specifications acceptable limit for the bypass leakage following a 
    surveillance is less than 10% of this design basis value. The most 
    recent bypass leakage value was approximately 2.5% for GGNS [....] 
    of the design allowable leakage rate limit for the limiting event. 
    EOI [Entergy Operations, Inc.] is committed to maintaining 
    programmatic and oversight controls that ensure that drywell bypass 
    leakage remains a small fraction of the design allowable leakage 
    limit.
        The drywell is typically exposed to essentially 0 psig during 
    normal plant operation and 3 psig during drywell bypass leak rate 
    testing. These pressures are considerably lower than the structural 
    integrity test pressure and are less likely to initiate a crack or 
    cause an existing crack to grow. Visual inspections of the 
    accessible drywell surfaces that have been performed since the 
    structural integrity tests have not revealed the presence of 
    additional cracking or other abnormalities. Therefore, additional 
    cracking of the drywell structure is not expected due to testing or 
    operation and, similar to the justification for the ten year 10 CFR 
    50 Appendix J Type A test interval, it is not considered credible 
    for the passive drywell structure to begin to leak sufficiently to 
    impact the design drywell bypass leakage limit.
        The primary containment's ability to perform its safety function 
    is fairly insensitive to the amount of drywell leakage, thereby 
    providing a margin to loss of the drywell safety function that is 
    not normally available for systems. This insensitivity is 
    demonstrated by the extremely high limiting event design basis 
    allowable leakage for the drywell (e.g., 35,000 scfm for GGNS 
    [....]). The limiting leakage is almost an order of magnitude higher 
    for other events. Additionally, an even higher allowable leakage can 
    be realistically accommodated by the primary containment due to the 
    margins in the containment design. Because of the margins available, 
    it will take valves in multiple penetration flow paths leaking 
    excessively to cause the primary containment to fail as a result of 
    overpressurization, the probability that drywell isolation valve 
    leakage will result in primary containment failure due to excessive 
    drywell leakage is not considered significant and this drywell/
    primary containment failure mode is not considered credible.
        The proposed Technical Specification changes have no significant 
    impact on the GGNS Individual Plant Examination (IPE) [....] 
    conducted per NRC Generic Letter 88-20. The IPEs considered 
    overpressurization failure of primary containment as part of the 
    primary containment performance assessment. Due to the magnitude of 
    acceptable drywell leakage and the extremely low probabilities of 
    achieving such leakage, primary containment failure due to 
    preexisting excessive drywell leakage was considered a non 
    significant contributor to primary containment failure. Primary 
    containment overpressurization failure can occur with or without 
    preexisting excessive drywell leakage in a severe accident. This is 
    due to physical phenomena associated with potentially extreme 
    environmental conditions inside primary containment following a 
    severe accident. However, the calculated frequency of such extreme 
    conditions is very small. The proposed changes do not impact the IPE 
    evaluated phenomena causing primary containment overpressurization 
    failure nor significantly increase the probability that the drywell 
    has preexisting excessive leakage and therefore would not contribute 
    to these accident scenarios.
        For the reasons discussed above, the proposed changes do not 
    have any significant risk impact to accidents previously evaluated 
    and do not significantly increase the consequences of an accident 
    previously evaluated. Additionally, drywell leakage is not the 
    initiator of any accident evaluated; therefore, changes in the 
    frequency of the surveillance for drywell leakage does not increase 
    the probability of any accident evaluated.
        Therefore, the proposed changes do not significantly increase 
    the probability or consequences of an accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The requested changes are either administrative changes which 
    clarify the format of the requirement or change the requirement to 
    match the design bases of the plant, a change which relocates the 
    requirement to the Technical Specification Bases, or a change in 
    surveillance interval. Each of these types of change are discussed 
    below:
        1. The administrative changes in the Technical Specification 
    requirements do not
    
    [[Page 25706]]
    
    involve a physical alteration of the plant (no new or different type 
    of equipment will be installed) nor does it change the methods 
    governing normal plant operation. Thus, this change does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        2. The proposed relocation of requirements does not involve a 
    physical alteration of the plant (no new or different type of 
    equipment will be installed) nor does it change the methods 
    governing normal plant operation. The proposed change will not 
    impose or eliminate any requirements. Adequate control of the 
    information will be maintained in the Technical Specification Bases. 
    Thus, the change proposed does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change modifies the surveillance frequency for 
    drywell bypass leakage and drywell air lock surveillances. The 
    changes only impact the test frequency and do not result in any 
    change in the response of the equipment to an accident. The changes 
    do not alter equipment design or capabilities. The changes do not 
    present any new or additional failure mechanisms. The drywell is 
    passive in nature and the surveillance will continue to verify that 
    its integrity has not deteriorated. Therefore, the proposed change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The requested changes are either administrative changes which 
    clarify the format of the requirement or change the requirement to 
    match the design bases of the plant, a change which relocates the 
    requirement to the Technical Specification Bases, or a change in 
    surveillance interval. Each of these types of changes are discussed 
    below:
        1. The administrative changes in the Technical Specification 
    requirements do not involve a physical alteration of the plant (no 
    new or different type of equipment will be installed) nor does it 
    change the methods governing normal plant operation. Thus, this 
    change does not cause a significant reduction in the margin of 
    safety.
        2. The relocation of requirements will not reduce a margin of 
    safety because it has no impact on any safety analysis assumptions. 
    In addition, the requirements to be transferred from the Technical 
    Specifications to the Technical Specifications Bases are the same as 
    the existing Technical Specifications. Since any future changes to 
    these requirements in the Technical Specifications Bases will be 
    evaluated per the requirements of 10 CFR 50.59, no reduction 
    (significant or insignificant) in a margin of safety will be 
    allowed.
        3. The proposed change modifies the surveillance frequency for 
    drywell bypass leakage and associated air lock surveillances. 
    Reliability of drywell integrity is evidenced by the measured 
    leakage rate during past drywell bypass leakage surveillances. 
    Appropriate design basis assumptions will be upheld, even when 
    combined with the complementary bypass leakage surveillances as 
    proposed. Drywell integrity will continue to be tested by means of 
    the proposed periodic drywell bypass leakage test, performance of 
    the drywell air lock door latching and interlock mechanism 
    surveillance, and performance of additional surveillances including 
    exercising of drywell isolation valves. The combination of these 
    surveillances will provide adequate assurance that drywell bypass 
    leakage will not exceed the design basis limit. Margins of safety 
    would not be reduced unless leakage rates exceeded the design 
    allowable drywell bypass leakage limit. Therefore, the proposed 
    change does not cause a significant reduction in the margin of 
    safety.
        Therefore, the proposed changes do not cause a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: August 11, 1995, as supplemented by 
    letter dated February 12, 1996.
        Description of amendment request: The proposed change will reduce 
    the minimum reactor coolant cold leg temperature from 544 Degrees F to 
    541 degrees F in Technical Specification Section 3.2.6, ``Reactor 
    Coolant Cold Leg Temperature.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change involves a 3 deg.F reduction in the minimum 
    core inlet temperature. This change will not have any impact on the 
    probability of occurrence of any accident documented in the FSAR.
        The impact of this change on the consequences of events 
    documented in the FSAR has been evaluated. The evaluation 
    demonstrated that most events are insensitive to the core inlet 
    temperature. The events that are impacted by lower core inlet 
    temperature are:
        Loss of condenser vacuum (LOCV),
        Part length CEA drop,
        Single CEA withdrawal within deadband, and
        CEA ejection.
        The LOCV event has been reanalyzed for the upcoming Cycle (Cycle 
    8) and the results indicate that the peak RCS pressure remains below 
    the acceptable limit (110% of the design pressure, i.e., 2750 psia). 
    The reactivity anomaly events (remaining events) will be reanalyzed 
    as part of COLSS/CPC setpoint calculations. These calculations will 
    be performed prior to Cycle 8 startup and will address the impact of 
    the 3 deg.F reduction on the minimum core inlet temperature. The 
    CPC/COLSS databases and/or addressable constants will be modified, 
    as needed due to proposed change, prior to cycle startup.
        A qualitative assessment of the impact of the proposed change on 
    the calculated LOCA blowdown loads that are applied to the major 
    NSSS components, their supports and the reactor vessel internals was 
    also performed. This assessment consisted of an evaluation of the 
    design margins on the major components and a determination of the 
    impact this lower temperature would have on those margins. The 
    evaluation concluded that the impact of a 3 deg.F cold leg 
    temperature reduction will be well within the current design 
    margins. Therefore, the proposed change will not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated.
        The proposed change to the minimum core inlet temperature does 
    not involve any change to any equipment or the manner in which the 
    plant will be operated. Since no hardware modifications or changes 
    in operation procedures will be made, the proposed change would not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated. Therefore, the proposed change 
    will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The impact of the proposed change on the Waterford 3 FSAR 
    analyses have been evaluated. The evaluation showed that the events 
    that were impacted were important with respect to RCS pressure and 
    fuel thermal limits. One of the events that was impacted by the 
    proposed change was the LOCV event. This event was analyzed and the 
    results showed that the peak RCS pressure remained below the 
    acceptable limit. The impact of this change on other events 
    (reactivity anomaly events) will be evaluated as part of the COLSS/
    CPC setpoint calculations and the COLSS/CPC databases and/or 
    addressable constants will modified as needed to account for any 
    adverse impact on the results of these events due to the proposed 
    change.
        The impact of this change on the Linear Heat Generation Rate 
    limits which varies as a function of the cold leg temperature, is 
    accounted for by Technical Specification 3.2.1, ``Linear Heat 
    Rate''. The impact of this change on LOCA blowdown loads were 
    evaluated to be insignificant compared to the
    
    [[Page 25707]]
    
    current design margins. Therefore, the proposed change will not 
    involve a significant reduction in a margin of safety, specifically 
    fuel thermal limits and RCS pressure limit.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Dates of amendment request: March 20, 1996, and April 23, 1996
        Description of amendment request: The licensee proposed to change 
    the Turkey Point Units 3 and 4 Technical Specifications (TS) to 
    relocate the requirements for surveillance testing of the water level 
    and pressure channel instrumentation for the reactor coolant system 
    accumulators and clarify the remaining TS surveillance tests. These 
    amendments also modify the existing action statements of TS 3.5.1 for 
    accumulators to reflect the requirements of NUREG-1431 by requiring a 
    72-hour period to restore boron concentration if it is not within the 
    limits, and a 1-hour period to restore any other condition rendering 
    the accumulators inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed amendments conform to the guidance given in 
    Enclosure 1 of the NRC GL [Generic Letter] 93-05. The overall 
    functional capabilities of the Emergency Core Cooling System (ECCS) 
    accumulators will not be modified by the proposed change. This 
    amendment will not involve a significant increase in the probability 
    or consequences of an accident previously evaluated for the 
    following reasons:
        1) The Water Level and Pressure Channel Instrumentation does not 
    perform a specific safety function, and merely provides an 
    indicating function. The instrumentation in no way affects the 
    capability of the accumulators to perform their respective safety 
    function.
        2) The changes in most of the ACTION statements are more 
    restrictive than current TS requirements due to the one hour vice 
    four hour completion time, and therefore will not increase the 
    probability or consequences of a previously evaluated accident. If 
    one accumulator is inoperable for a reason other than boron 
    concentration, the accumulator must be returned to OPERABLE status 
    within 1 hour. In this condition, the required contents of three 
    accumulators cannot be assumed to reach the core during a Loss Of 
    Coolant Accident (LOCA). Due to the severity of the consequences 
    should a LOCA occur in these conditions, the 1 hour completion time 
    to open the valve, remove power to the valve, or restore the proper 
    water volume or nitrogen cover pressure ensures that prompt action 
    will be taken to return the inoperable accumulator to OPERABLE 
    status. The completion time minimizes the potential for exposure of 
    the plant to a LOCA under these conditions. The 1 hour requirement 
    for restoring a closed isolation valve is merely a clarification of 
    the existing ``immediate'' time requirement.
        3) In the case of low-out-of-specification boron concentration 
    in one accumulator, it must be returned to within the limits within 
    72 hours. In this condition, ability to maintain subcriticality or 
    minimum boron precipitation time may be reduced. The boron in the 
    accumulators contributes to the assumption that the combined ECCS 
    water in the partially recovered core during the early reflooding 
    phase of a large break LOCA is sufficient to keep that portion of 
    the core subcritical. One accumulator below the minimum boron 
    concentration limit, however, will have no effect on available ECCS 
    water and an insignificant effect on core subcriticality during 
    reflood. Boiling of ECCS water in the core during reflood 
    concentrates boron in the saturated liquid that remains in the core. 
    In addition, current Turkey Point analysis demonstrate that the 
    accumulators discharge only a small amount following a large main 
    steam line break. Therefore, their impact on boron concentration in 
    the reactor coolant system is minor and not a design limiting event. 
    Thus, 72 hours is allowed to return the boron concentration to 
    within limits and does not increase the probability or consequences 
    of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The use of the modified specifications can not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated since the proposed amendments will not change 
    the physical plant or the modes of plant operation defined in the 
    facility operating license. No new failure mode is introduced due to 
    the surveillance changes and clarifications, since the proposed 
    changes do not involve the addition or modification of equipment nor 
    do they alter the design or operation of affected plant systems.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The operating limits and functional capabilities of the affected 
    system are unchanged by the proposed amendment. The modified 
    specifications which remove surveillance requirements from the TS to 
    plant procedures are consistent with the NRC GL 93-05 line-item 
    improvement guidance do not significantly reduce any of the margins 
    of safety even though the amount of surveillances is decreased. The 
    modification of the existing ACTION Statements do not have an 
    adverse on [sic] affect on the margin of safety for the following 
    reasons:
        1) The SI [Safety Injection] Accumulator Water Level and 
    Pressure Channel instrumentation performs no safety function.
        2) The changes in ACTION statements a) and b) are for the most 
    part more restrictive than existing TS requirements, the reason 
    being the removal of instrumentation requirements for operability.
        3) In the case of low-out-of-specification boron concentration 
    in one accumulator, the requirement will be less restrictive, but 
    the low boron concentration in one accumulator will have no effect 
    on available ECCS water and an insignificant effect on core 
    subcriticality during reflood and therefore will not significantly 
    reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: Frederick J. Hebdon
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of amendment request: April 19, 1996
        Description of amendment request: The proposed amendment would 
    include revisions to Technical Specification (TS) 3.3.6.1, ``Primary 
    Containment and Drywell Isolation Instrumentation; TS 
    3.3.6.2, ``Secondary Containment Isolation Instrumentation; 
    TS 3.3.7.1, ``Control Room Ventilation System 
    Instrumentation; TS 3.6.1.2, ``Primary Containment Air 
    Locks; TS 3.6.1.3,
    
    [[Page 25708]]
    
    ``Primary Containment Isolation Valves; TS 3.6.4.1, 
    ``Secondary Containment; TS 3.6.4.2, ``Secondary Containment 
    Isolation Dampers; TS 3.6.4.3, ``Standby Gas 
    Treatment; TS 3.7.3, ``Control Room Ventilation; 
    and TS 3.7.4, ``Control Room AC System.'' These TSs would be revised to 
    eliminate CORE ALTERATIONS as an applicable condition for which the 
    associated Limiting Conditions for Operation (LCO) must be met. 
    Consistent changes are also proposed for the associated ACTIONS in each 
    of these LCOs, to reflect the changes in the applicable conditions. The 
    intent of these proposed changes is to allow certain activities such as 
    control rod venting, which is considered a CORE ALTERATION in MODE 5, 
    to be performed without the requirements of the identified LCOs being 
    met.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed changes eliminate CORE ALTERATIONS as an 
    applicable condition requiring operability of the primary and 
    secondary containment and control room ventilation system. As stated 
    in the BASES for the associated Technical Specifications, 
    operability of these systems is primarily required for mitigation of 
    the design basis accident - fuel handling accident (DBA-FHA) and 
    design basis accident - loss of coolant accident (DBA-LOCA). The 
    performance of CORE ALTERATIONS alone is neither a precursor to, nor 
    a condition during which these DBAs are postulated to occur. The 
    proposed changes only delete CORE ALTERATIONS as an applicable 
    condition for the affected Technical Specifications. All other 
    applicable MODES or specified conditions, including operations with 
    the potential for draining the reactor vessels (OPDRVs) and the 
    movement of irradiated fuel assemblies within the primary or 
    secondary containment, remain unchanged. Further, the limitations 
    placed on the handling of light loads are also unchanged. The 
    Technical Specifications (and the separate requirements imposed on 
    the handling of light loads) will thus continue to require that 
    systems or functions designed to mitigate design-basis/previously 
    evaluated accidents are OPERABLE during the relevant operating MODES 
    or conditions. On the basis of the above, it is concluded that the 
    requested amendment will not increase the probability or 
    consequences of any accident previously evaluated.
        2. The proposed changes do not involve any modification to the 
    plant design or to the operation of plant systems (except to 
    determine when certain analyzed accident-mitigating systems or 
    features are required to be OPERABLE). The failure modes considered 
    for the proposed changes are the same as those previously 
    considered, therefore, it can be concluded that no new failure modes 
    will be created. On this basis, the proposed amendment will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The changes being made to eliminate CORE ALTERATIONS as an 
    applicable condition for which certain LCOs must be met, do not 
    eliminate the requirements for operability of those systems or 
    features assumed to mitigate design-basis or analyzed accidents 
    during the applicable MODES when such systems or features are 
    assumed to be available for performing their mitigating function. 
    The safety margins assumed or established by the accident analyses 
    for those design-basis events (as described in the accident analyses 
    of the Clinton Power Station Updated Final Safety Analysis Report) 
    therefore remain unchanged. Further, the proposed changes do not 
    impact the controls imposed on the handling of light loads 
    (including unirradiated fuel assemblies) for ensuring that such 
    activities cannot result in an event that yields consequences more 
    severe than those calculated for the DBA-FHA. With respect to 
    reactivity concerns during refueling operations (MODE 5), all 
    systems or features required to be OPERABLE for precluding 
    inadvertent criticality and monitoring reactivity changes will 
    continue to be required OPERABLE as per the current Technical 
    Specification requirements. The deletion of CORE ALTERATIONS as an 
    applicable condition only applies to the noted systems which do not 
    contribute to precluding reactivity events. Based on the above, the 
    proposed changes do not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
        Attorney for licensee: Leah Manning Stetener, Vice President, 
    General Counsel, and Corporate Secretary, 500 South 27th Street, 
    Decatur, Illinois 62525
        NRC Project Director: Gail H. Marcus
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket 
    No. 50-461, Clinton Power Station, Unit No. 1, DeWitt County, 
    Illinois
    
        Date of amendment request: May 1, 1996
        Description of amendment request: The proposed amendment would 
    revise the Clinton Power Station (CPS) Operating License and Technical 
    Specifications (TS) to implement 10 CFR Part 50, Appendix J - Option B, 
    by referring to Regulatory Guide 1.163, ``Performance-Based Containment 
    Leak-Test Program.'' Specifically, changes would be made to paragraph 
    2.D of the Operating License; TS Section 1.1, ``Definitions;'' TS 
    3.6.1.1, ``Primary Containment;'' TS 3.6.1.1, ``Primary Containment Air 
    Locks;'' TS 3.6.1.3, ``Primary Containment Isolation Valves (PCIVs);'' 
    and TS Section 5.5, ``Programs and Manuals.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change implements new Option B of 10 CFR 50 
    Appendix J for performance-based primary containment leakage 
    testing. The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any parameters or conditions that contribute to the 
    initiation of any accidents previously evaluated. Thus, the proposed 
    change cannot increase the probability of any accident previously 
    evaluated.
        The proposed change potentially affects the leak-tight integrity 
    of the primary containment structure which is designed to mitigate 
    the consequences of a loss-of-coolant accident (LOCA) by limiting 
    the release of fission products contained in the post-LOCA primary 
    containment atmosphere. Functional integrity of the primary 
    containment must be maintained during and following the peak 
    transient pressures and temperatures that may result from a LOCA. 
    Because the proposed change does not alter the plant design, 
    including the primary containment and primary containment 
    penetrations, and because it only affects the frequency of measuring 
    Type A, B, and C leakage without changing the acceptance criteria 
    for the Type A, B, and C leakage rate tests, the proposed change 
    does not directly result in an increase in the primary containment 
    leakage. However, decreasing the test frequency can increase the 
    probability that an increase in primary containment leakage could go 
    undetected for an extended period of time. To minimize that 
    probability, test intervals will be established based on the 
    performance history of components being tested.
        NUREG-1493, ``Performance-Based Containment Leak-Test Program,'' 
    provides the technical basis for the NRC's rulemaking to revise 
    primary containment leakage testing requirements for nuclear power 
    reactors in 10 CFR 50, Appendix J. NUREG-1493 documents the NRC's 
    determination that the effect of primary containment leakage on 
    overall accident risk is minimal since risk is dominated by accident 
    sequences that result in failure of bypass of primary containment. 
    NUREG-1493 also documents that increasing the Type A leakage test 
    intervals would have a minimal impact on public risk, and that Type 
    B and C tests can identify the vast majority (greater than ninety 
    five percent) of all leakage paths. Therefore, performance-based 
    alternatives to current local leakage-testing requirements are 
    feasible without significant risk impacts.
    
    [[Page 25709]]
    
        Based on the above, IP has concluded that the proposed change 
    will not result in a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that could contribute to 
    initiation of any accidents. This change involves the reduction of 
    Type A, B, and C test frequency. Except for the method of defining 
    the test frequency, the methods for performing the actual tests are 
    not changed. No new accident modes are created by extending the 
    testing intervals. No safety-related equipment or safety functions 
    are altered as a result of this change. Thus, extending the test 
    frequency has no influence on, nor does it contribute to the 
    possibility of a new or different kind of accident or malfunction 
    from those previously analyzed.
        Based on the above, IP has concluded that the proposed change 
    will not create the possibility of a new or different kind of 
    accident not previously evaluated.
        3. The request does not involve a significant reduction in a 
    margin to safety. The proposed change only affects the frequency of 
    the Type A, B, and C testing. Except for the method of defining the 
    test frequency, the methods for performing the actual tests are not 
    changed. However, the proposed change can increase the probability 
    that an increase in primary containment leakage could go undetected 
    for an extended period of time. NUREG-1493 has determined that under 
    several different accident scenarios, the increased risk of 
    radioactivity release from primary containment is negligible with 
    the implementation of these proposed changes.
        The margin of safety that has the potential of being impacted by 
    the proposed change involves the offsite dose consequences of 
    postulated accidents which are directly related to the rate of 
    primary containment leakage. The primary containment isolation 
    system is designed to limit leakage to La, which is defined by 
    the CPS Technical Specifications to be 0.65% of primary containment 
    air weight per day at the calculated peak containment internal 
    pressure for the design basis loss of coolant accident (Pa). 
    The limitation on the rate of primary containment leakage is 
    designed to ensure that the total leakage volume will not exceed the 
    value assumed in the accident analyses at the peak accident pressure 
    (Pa). The margin of safety for the offsite dose consequences of 
    postulated accidents directly related to the primary containment 
    leakage rate is maintained by continuing to meet the 1.0 La 
    acceptance criteria. The La value is not being modified by this 
    proposed change.
        Except for the method of defining the test frequency, no change 
    in the method of testing is being proposed. The Type A, B, and C 
    tests will continue to be done at full pressure (Pa) or 
    greater. Other programs are in place to ensure that proper 
    maintenance and repairs are performed during the service life of the 
    primary containment and systems and components penetrating the 
    primary containment.
        As a result, IP has concluded that the proposed change will not 
    result in a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727
        Attorney for licensee: Leah Manning Stetener, Vice President, 
    General Counsel, and Corporate Secretary, 500 South 27th Street, 
    Decatur, Illinois 62525
        NRC Project Director: Gail H. Marcus
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: January 25, 1996
        Description of amendment request: The amendment proposes to extend 
    instrumentation and miscellaneous surveillance test intervals (STI) to 
    support 24-month operating cycles. Additionally, this application 
    proposes: (1) to revise the Trip Level Settings for Emergency Bus Loss 
    of Voltage and Degraded Voltage Instrumentation, (2) to revise the 
    Reactor Protection System (RPS) Normal Supply Electrical Protection 
    Assembly (EPA) Undervoltage Trip Setpoint, and (3) to make editorial 
    revisions, clarification and Bases changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed STI changes evaluated in Section IV.A do not 
    involve any physical changes to the plant, do not alter the way 
    these systems function, and will not degrade the performance of the 
    plant safety systems. Proposed instrument setpoint changes ensure 
    that plant safety limits are not exceeded due to instrument drift 
    predicted for the longer calibration interval. The type of testing 
    and the corrective actions required if the subject surveillances 
    fail remains the same. The proposed changes do not adversely affect 
    the reliability of these systems or affect the ability of the 
    systems to meet their design objectives. A historical review of 
    surveillance test results supports these conclusions.
        The Trip Level Setpoint changes evaluated in Section IV.B ensure 
    that the related systems perform as assumed in the transient and 
    accident analysis by ensuring that plant safety limits are not 
    exceeded due to instrument drift predicted for the longer 
    calibration interval. The changes do not alter the system function, 
    and will not degrade the performance of plant safety systems. The 
    proposed Trip Level Setting changes do not adversely affect the 
    reliability of these systems or adversely affect the ability of 
    these systems to meet their design objectives.
        The editorial, clarification and Bases changes evaluated in 
    Section IV.C propose enhancements that clarify the Technical 
    Specifications requirements and are editorial in nature. These 
    changes do not alter any Technical Specification requirement, do not 
    involve physical changes to the plant, or alter any operational 
    setpoints. There are no safety implications in these proposed 
    changes.
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed STI changes evaluated in Section IV.A do not modify 
    the design or operation of the plant, therefore, no new failure 
    modes are introduced. Proposed instrument setpoint changes ensure 
    that plant safety limits are not exceeded due to instrument drift 
    resulting from the longer calibration interval. No changes are 
    proposed to the type and method of testing performed, only to the 
    length of the surveillance test interval. Past equipment performance 
    and on-line testing indicate that longer test intervals will not 
    degrade these systems. A historical review of surveillance test 
    results supports these conclusions.
        The Trip Level Setpoint changes evaluated in Section IV.B ensure 
    that the related systems perform as assumed in the transient and 
    accident analysis by ensuring that plant safety limits are not 
    exceeded due to instrument drift predicted for the longer 
    calibration interval. The changes do not alter the system function, 
    introduce any new failure modes, and will not degrade the 
    performance of plant safety systems. The proposed Trip Level Setting 
    changes do not adversely affect the reliability of these systems or 
    adversely affect the ability of these systems to meet their design 
    objectives.
        The editorial, clarification and Bases changes evaluated in 
    Section IV.C propose enhancements that clarify the Technical 
    Specifications requirements and are editorial in nature. These 
    changes do not alter any Technical Specification requirement, do not 
    involve physical changes to the plant, or alter any operational 
    setpoints. There are no safety implications in these proposed 
    changes.
        3. involve a significant reduction in a margin of safety.
        Although the proposed STI changes evaluated in Section IV.A will 
    result in an increase in the interval between surveillance tests, 
    the impact on system reliability is minimal. This is based on more 
    frequent on-line testing and the redundant design of the evaluated 
    systems. A review of past surveillance history has shown no evidence
    
    [[Page 25710]]
    
    of failures which would significantly impact the reliability of 
    these systems. Operation of the plant remains unchanged by these 
    proposed STI extensions. The assumptions in the Plant Licensing 
    Basis are not adversely impacted. Therefore, the proposed changes do 
    not result in a significant reduction in the margin of safety.
        The Trip Level Setpoint changes evaluated in Section IV.B ensure 
    that the related systems perform as assumed in the transient and 
    accident analysis by ensuring that plant safety limits are not 
    exceeded due to instrument drift predicted for the longer 
    calibration interval. The changes do not alter the system function, 
    introduce any new failure modes, and will not degrade the 
    performance of plant safety systems. The proposed Trip Level Setting 
    changes do not adversely affect the reliability of these systems or 
    adversely affect the ability of these systems to meet their design 
    objectives.
        The editorial, clarification and Bases changes evaluated in 
    Section IV.C propose enhancements that clarify the Technical 
    Specifications requirements and are editorial in nature. These 
    changes do not alter any Technical Specification requirement, do not 
    involve physical changes to the plant, or alter any operational 
    setpoints. There are no safety implications in these proposed 
    changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Susan Frant Shankman, Acting
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: April 24, 1996
        Description of amendment request: This amendment proposes to 
    relocate Technical Specification (TS) 3.11.B/4.11.B ``Crescent Area 
    Ventilation'' and associated Bases from the TS to an Authority 
    controlled procedure.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment will not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, based on the following:
        (1) These changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated 
    because:
        No modifications, no changes to operating procedure 
    requirements, and no reduction in equipment reliability are being 
    made as a result of these changes. Operating limitations will 
    continue to be imposed, and required surveillance will continue to 
    be performed in accordance with regulations, and written procedures 
    and instructions that are auditable by the [Nuclear Regulatory 
    Commission] NRC. Crescent Area Ventilation operability and testing 
    requirements will continue to be an integral part of FitzPatrick 
    plant operation.
        Although future changes to the Crescent Area Ventilation system 
    will no longer be controlled by 10 CFR 50.90, proposed changes will 
    be evaluated under 10 CFR 50.59 and plant procedures. Programmatic 
    controls will continue to assure that Crescent Area Ventilation 
    system changes will not adversely affect [Emergency Core Cooling 
    System] ECCS or [Reactor Core Isolation Cooling] RCIC system 
    operability. As such, there is no significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) These changes do not create the possibility of a new or 
    different type of accident previously evaluated because:
        No modifications, no changes to operating procedure 
    requirements, and no reduction in equipment reliability are being 
    made as a result of these changes. Compliance with Crescent Area 
    Ventilation system operability and surveillance requirements will be 
    assured by maintaining them in an Authority controlled procedure. 
    Changes to the Crescent Area Ventilation system will be subject to 
    the requirements of 10 CFR 50.59. Therefore, the proposed changes do 
    not introduce any failure mechanism of a different type than those 
    previously evaluated since there are no changes being made to the 
    facility and do not create the possibility of a new or different 
    type of accident previously evaluated.
        (3) The proposed amendment does not involve a reduction in a 
    margin of safety because:
        The Crescent Area Ventilation system supports Core Spray, [Low 
    Pressure Coolant Injection] LPCI mode of [Residual Heat Removal] 
    RHR, containment cooling mode of RHR, [High Pressure Coolant 
    Injection] HPCI, and RCIC operability, and Crescent Area Ventilation 
    system inoperability does affect these systems. As a result, the 
    requirement for Crescent Area Ventilation to be operable for these 
    systems to be considered operable is implicit in TS Sections 3.5.A, 
    3.5.B, 3.5.C, 3.5.E, and the definition of OPERABLE contained in TS 
    Section 1.0.J. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Susan Frant Shankman, Acting
    
    Public Service Electric & Gas Company, Docket No. 50-311, Salem 
    Nuclear Generating Station, Unit No. 2, Salem County, New Jersey
    
        Date of amendment request: May 7, 1996
        Description of amendment request: The proposed amendment involves a 
    one-time change to Technical Specification (TS) 3/4.7.6, ``Control Room 
    Emergency Air Conditioning System.'' The change would permit refueling 
    of Salem, Unit 2, with the Control Room Emergency Air Conditioning 
    System (CREACS) inoperable in Modes 5 and 6. The change will expire 
    after the completion of the Control Room and CREACS upgrade, which is 
    currently in progress, and the restart and entry into Mode 4 of Unit 2 
    from the current outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The CREACS is not an accident initiator. CREACS functions post-
    accident to provide cooling for Control Room equipment and 
    habitability for operations personnel. Therefore, CREACS has no 
    influence on the probability of any of the previously evaluated 
    accidents or the other events evaluated as listed below.
        Event
        Fuel Handling Accident (Salem)
        Waste Gas or Volume Control Tank Failures
        Uncontrolled Boron Dilution
        Loss of Offsite Power
        Fuel Handling Accident (Hope Creek)
        Liquid and Gaseous Waste Releases (Hope Creek)
        Loss of Coolant Accident (LOCA) (Hope Creek)
        Chemical Storage
        Barge Collision
        Control Room Internal and External Fire
        Loss of Spent Fuel Pool Cooling
        Loss of Decay Heat Removal
        The Control Area Air Conditioning System (CAACS) and other 
    measures will be
    
    [[Page 25711]]
    
    available to maintain Control Room Envelope (CRE) ambient 
    temperatures and habitability.
        The proposed one-time change does not impact the consequences of 
    an accident previously evaluated based on the following discussions.
        The fuel has decayed to such low levels for more than six months 
    that doses associated with the fuel handling accident are well 
    within the limits of GDC [General Design Criteria] 19. There is 
    insufficient activity remaining in either gaseous waste storage or 
    liquid waste storage to force a Control Room evacuation. In the 
    event of a Loss of Offsite Power (LOOP), uncontrolled boron dilution 
    event, loss of spent fuel pool cooling or loss of decay heat 
    removal, CREACS is not required in Modes 5 or 6 to mitigate the 
    consequences of this event and CRE habitability will be maintained.
        For a Hope Creek fuel handling accident, gaseous radwaste 
    release of LOCA, dose to Salem Control Room personnel will not 
    exceed GDC 19 limits. PSE&G [Public Service Electric & Gas] will 
    maintain the CAACS [Control Area Air Conditioning System] outside 
    air intakes either isolated or capable of being isolated in the 
    event of a Hope Creek LOCA. The Hope Creek Event Classification 
    Guide (ECG) requires notification of the Salem Control Room in the 
    event of an emergency that has the potential to result in a 
    radioactive release. The Salem Control Room will isolate the outside 
    air intakes if isolation has not already been accomplished.
        For the other events evaluated, the need for evacuation is not 
    considered credible for any event with the exception of an internal 
    or external fire. However, the possibility of evacuation of the CRE 
    in the event of an internal or external fire would be no different 
    whether or not CREACS is operating. In the event of an internal 
    fire, CAACS will remain in operation to provide purging of the CRE. 
    For the case of a possible external fire, the need for evacuation is 
    not considered credible because of the short duration of the CREACS 
    outage and improbability of the factors which are necessary to 
    require an evacuation of the Control Room (i.e. wind direction, wind 
    speed, amount of smoke). If an external fire is detected, operator 
    action will be taken to isolate the CRE from outside air while CAACS 
    remains available. In the unlikely event that the Control Room would 
    become uninhabitable due to smoke in the atmosphere, evacuation 
    procedures would be followed as in the case of the internal fire.
        The one chemical storage type event which might impact the 
    Control Room, rupture of an ammonium hydroxide tanker, is precluded 
    by administrative controls such that no ammonium hydroxide tanker 
    deliveries will be allowed during the system upgrade period.
        The CAACS will maintain the current design function and TS Bases 
    requirements of the CREACS that the ambient air temperature does not 
    exceed the allowable temperature for continuous duty rating for 
    equipment and instrumentation cooled by the system for the combined 
    CRE. The CAACS will be maintained functional while modification to 
    the CREACS is ongoing to provide cooling during normal operation and 
    under postulated accident conditions. Should the temperature in the 
    CRE exceed allowable levels (85 Degrees F), administrative controls 
    will be in place to require restoration of the temperature to within 
    acceptable levels using CAACS, and prevent any Core Alteration 
    activities or positive reactivity changes until the temperature is 
    restored to acceptable levels.
        Therefore, the proposed one-time TS change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The CREACS is not an accident initiator. CREACS functions post-
    accident to provide cooling for Control Room equipment and 
    habitability for operations personnel. Therefore, CREACS 
    inoperability during Modes 5 and 6 will not result in the creation 
    of a new or different kind of accident from any accident previously 
    evaluated. All pertinent accidents have been assessed and no other 
    scenarios dealing with fuel movement, or the need for an operable 
    CREACS in Mode 5 or 6, have been deemed credible.
        Therefore, the proposed one-time change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed one-time change does not significantly reduce the 
    margin of safety as defined in the Bases for the TS because (1) 
    there is no credible event as analyzed in Salem UFSAR [updated final 
    safety analysis report] Chapter 15 which can cause an unacceptable 
    environment in the CRE since the fuel has been decaying for at least 
    six months, (2) fuel movement inside the Fuel Handling Building 
    (FHB) is restricted in accordance with plant TS unless FHB 
    ventilation is operable, (3) dose to Salem control room personnel 
    from a potential Hope Creek fuel handling accident, gaseous radwaste 
    release or Loss of Coolant Accident will not exceed GDC 19 limits 
    (4) the one event which might impact the Control Room, rupture of an 
    ammonium hydroxide tanker, is precluded by administrative controls 
    such that no ammonium hydroxide tanker deliveries will be allowed 
    during the CREACS upgrade period, and (5) in the unlikely event that 
    Control Room evacuation is required, there is no impact on operator 
    ability to mitigate the consequences of an accident in the current 
    plant configuration.
        Therefore, the proposed one-time TS change does not involve a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Southern Nuclear Operating Company, Inc., Docket No. 50-364, Joseph 
    M. Farley Nuclear Plant, Unit 2, Houston County, Alabama
    
        Date of amendment request: March 29, 1996
        Description of amendment request: The proposed amendment would 
    revise Technical Specification 3/4.4.6 ``Steam Generators'' and its 
    associated Bases. Specifically, the steam generator repair limit would 
    be modified to clarify that the appropriate method for determining 
    serviceability for tubes with outside diameter stress corrosion 
    cracking at the tube support plate is by a methodology that more 
    reliably assesses structural integrity. This amendment request is in 
    accordance with NRC's Generic Letter 95-05, ``Voltage-Based Repair 
    Criteria for Westinghouse Steam Generator Tubes Affected by Outside 
    Diameter Stress Corrosion Cracking.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of Farley units in accordance with the proposed 
    license amendment does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Testing of model boiler specimens for free standing tubes at 
    room temperature conditions shows burst pressures as high as 
    approximately 5000 psi for indications of outer diameter stress 
    corrosion cracking with voltage measurements as high as 26.5 volts. 
    Burst testing performed on pulled tubes, including tubes pulled from 
    Farley Unit 2, with up to 7.5 volt indications show burst pressures 
    in excess of 5300 psi at room temperature. As stated earlier, tube 
    burst criteria are inherently satisfied during normal operating 
    conditions by the presence of the tube support plate. Furthermore, 
    correcting for the effects of temperature on material properties and 
    minimum strength levels (as the burst testing was done at room 
    temperature), tube burst capability significantly exceeds the R.G. 
    [Regulatory Guide] 1.121 criterion requiring the maintenance of a 
    margin of 1.43 times the steam line break pressure differential on 
    tube burst if through-wall cracks are present without regard to the 
    presence of the tube support plate. Considering the existing data 
    base, this criterion is satisfied with bobbin coil indications with 
    signal amplitudes over twice the 2.0 volt voltage-based repair 
    criteria, regardless of the indicated depth measurement. This 
    structural limit is based on a lower 95% confidence level limit of 
    the
    
    [[Page 25712]]
    
    data at operating temperatures. The 2.0 volt criterion provides a 
    conservative margin of safety to the structural limit considering 
    expected growth rates of outside diameter stress corrosion cracking 
    at Farley. Alternate crack morphologies can correspond to a voltage 
    so that a unique crack length is not defined by a burst pressure to 
    voltage correlation. However, relative to expected leakage during 
    normal operating conditions, no field leakage has been reported from 
    tubes with indications with a voltage level of under 7.7 volts for a 
    3/4 inch tube with a 10 volt correlation to 7/8 inch tubing (as 
    compared to the 2.0 volt proposed voltage-based tube repair limit). 
    Thus, the proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident.
        Relative to the expected leakage during accident condition 
    loadings, the accidents that are affected by primary-to-secondary 
    leakage and steam release to the environment are Loss of External 
    Electrical Load and/or Turbine Trip, Loss of All AC Power to Station 
    Auxiliaries, Major Secondary System Pipe Failure, Steam Generator 
    Tube Rupture, Reactor Coolant Pump Locked Rotor, and Rupture of a 
    Control Rod Drive Mechanism Housing. Of these, the Major Secondary 
    System Pipe Failure is the most limiting for Farley in considering 
    the potential for off-site doses. The offsite dose analyses for the 
    other events which model primary-to secondary leakage and steam 
    releases from the secondary side to the environment assume that the 
    secondary side remains intact. The steam generator tubes are not 
    subjected to a sustained increase in differential pressure, as is 
    the case following a steam line break event. This increase in 
    differential pressure is responsible for the postulated increase in 
    leakage and associated offsite doses following a steam line break 
    event. In addition, the steam line break event results in a bypass 
    of containment for steam generator leakage. Upon implementation of 
    the voltage-based repair criteria, it must be verified that the 
    expected distributions of cracking indications at the tube support 
    plate intersections are such that primary-to-secondary leakage would 
    result in site boundary dose within the current licensing basis. 
    Data indicate that a threshold voltage of 2.8 volts could result in 
    through-wall cracks long enough to leak at steam line break 
    conditions. Application of the proposed repair criteria requires 
    that the current distribution of a number of indications versus 
    voltage be obtained during the refueling outages. The current 
    voltage is then combined with the rate of change in voltage 
    measurement and a voltage measurement uncertainty to establish an 
    end of cycle voltage distribution and, thus, leak rate during steam 
    line break pressure differential. The leak rate during a steam line 
    break is further increased by a factor related to the probability of 
    detection of the flaws. If it is found that the potential steam line 
    break leakage for degraded intersections planned to be left in 
    service coupled with the reduced allowable specific activity levels 
    result in radiological consequences outside the current licensing 
    basis, then additional tubes will be plugged or repaired to reduce 
    steam line break leakage potential to within the acceptance limit. 
    Thus, the consequences of the most limiting design basis accident 
    are constrained to present licensing basis limits.
        2) The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Implementation of the proposed voltage-based tube support plate 
    elevation steam generator tube repair criteria does not introduce 
    any significant changes to the plant design basis. Use of the 
    criteria does not provide a mechanism that could result in an 
    accident outside of the region of the tube support plate elevations. 
    Neither a single or multiple tube rupture event would be expected in 
    a steam generator in which the repair criteria have been applied 
    during all plant conditions. The bobbin probe signal amplitude 
    repair criteria are established such that operational leakage or 
    excessive leakage during a postulated steam line break condition is 
    not anticipated. Southern Nuclear has previously implemented a 
    maximum leakage limit of 150 gpd per steam generator. The R.G. 1.121 
    criterion for establishing operational leakage limits that require 
    plant shutdown are based upon leak-before-break considerations to 
    detect a free span crack before potential tube rupture. The 150 gpd 
    limit provides for leakage detection and plant shutdown in the event 
    of the occurrence of an unexpected single crack resulting in leakage 
    that is associated with the longest permissible crack length. R.G. 
    1.121 acceptance criteria for establishing operating leakage limits 
    are based on leak-before-break considerations such that plant 
    shutdown is initiated if the leakage associated with the longest 
    permissible crack is exceeded. The longest permissible crack is the 
    length that provides a factor of safety of 1.43 against bursting at 
    steam line break pressure differential. A voltage amplitude of 
    approximately 9 volts for typical outside diameter stress corrosion 
    cracking corresponds to meeting this tube burst requirement at the 
    95% prediction interval on the burst correlation. Alternate crack 
    morphologies can correspond to a voltage so that a unique crack 
    length is not defined by the burst pressure versus voltage 
    correlation. Consequently, a typical burst pressure versus through-
    wall crack length correlation is used below to define the ``longest 
    permissible crack'' for evaluating operating leakage limits.
        The single through-wall crack lengths that result in tube burst 
    at 1.43 times steam line break pressure differential and steam line 
    break conditions are about 0.54 inch and 0.84 inch, respectively. 
    Normal leakage for these crack lengths would range from about 0.4 
    gallons per minute to 4.5 gallons per minute, respectively, while 
    lower 95% confidence level leak rates would range from about 0.06 
    gallons per minute to 0.6 gallons per minute, respectively.
        An operating leak rate of 150 gpd per steam generator has been 
    implemented. This leakage limit provides for detection of 0.4 inch 
    long cracks at nominal leak rates and 0.6 inch long cracks at the 
    lower 95% confidence level leak rates. Thus, the 150 gpd limit 
    provides for plant shutdown prior to reaching critical crack lengths 
    for steam line break conditions at leak rates less than a lower 95% 
    confidence level and for three times normal operating pressure 
    differential at less than nominal leak rates.
        Considering the above, the implementation of voltage-based 
    plugging criteria will not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3) The proposed license amendment does not involve a significant 
    reduction in margin of safety.
        The use of the voltage-based tube support plate elevation repair 
    criteria is demonstrated to maintain steam generator tube integrity 
    commensurate with the requirements of Generic Letter 95-05 and R.G. 
    1.121. R.G. 1.121 describes a method acceptable to the NRC staff for 
    meeting GDC [Generic Design Criteria] 2, 14, 15, 31, and 32 by 
    reducing the probability of the consequences of steam generator tube 
    rupture. This is accomplished by determining the limiting conditions 
    of degradation of steam generator tubing, as established by 
    inservice inspection, for which tubes with unacceptable cracking 
    should be removed from service. Upon implementation of the criteria, 
    even under the worst case conditions, the occurrence of outside 
    diameter stress corrosion cracking at the tube support plate 
    elevations is not expected to lead to a steam generator tube rupture 
    event during normal or faulted plant conditions. The most limiting 
    effect would be a possible increase in leakage during a steam line 
    break event. Excessive leakage during a steam line break event, 
    however, is precluded by verifying that, once the criteria are 
    applied, the expected end of cycle distribution of crack indications 
    at the tube support plate elevations would result in minimal, and 
    acceptable primary to secondary leakage during the event and, hence, 
    help to demonstrate radiological conditions are less than an 
    appropriate fraction of the 10 CFR [Part] 100 guideline.
        The margin to burst for the tubes using the voltage-based repair 
    criteria is comparable to that currently provided by existing 
    Technical Specifications.
        In addressing the combined effects of LOCA [loss-of-coolant 
    accident] + SSE [safe-shutdown earthquake] on the steam generator 
    component (as required by GDC 2), it has been determined that tube 
    collapse may occur in the steam generators at some plants. This is 
    the case as the tube support plates may become deformed as a result 
    of lateral loads at the wedge supports at the periphery of the plate 
    due to either the LOCA rarefaction wave and/or SSE loadings. Then, 
    the resulting pressure differential on the deformed tubes may cause 
    some of the tubes to collapse.
        There are two issues associated with steam generator tube 
    collapse. First, the collapse of steam generator tubing reduces the 
    RCS [reactor coolant system] flow area through the tubes. The 
    reduction in flow area increases the resistance to flow of steam 
    from the core during a LOCA which, in turn, may potentially increase 
    Peak Clad Temperature (PCT). Second, there is a potential the 
    partial through-wall cracks in tubes could progress to through-wall 
    cracks during tube deformation or collapse or that short through-
    
    [[Page 25713]]
    
    wall indications would leak at significantly higher leak rates than 
    included in the leak rate assessments.
        Consequently, a detailed leak-before-break analysis was 
    performed and it was concluded that the leak-before-break 
    methodology (as permitted by GDC 4) is applicable to the Farley 
    reactor coolant system primary loops and, thus, the probability of 
    breaks in the primary loop piping is sufficiently low that they need 
    not be considered in the structural design basis of the plant. 
    Excluding breaks in the RCS primary loops, the LOCA loads from the 
    large branch line breaks were analyzed at Farley and were found to 
    be of insufficient magnitude to result in steam generator tube 
    collapse or significant deformation.
        Regardless of whether or not leak-before-break is applied to the 
    primary loop piping at Farley, any flow area reduction is expected 
    to be minimal (much less than 1%) and PCT margin is available to 
    account for this potential effect. Based on analyses' results, no 
    tubes near wedge locations are expected to collapse or deform to the 
    degree that secondary to primary in-leakage would be increased over 
    current expected levels. For all other steam generator tubes, the 
    possibility of secondary-to-primary leakage in the event of a LOCA + 
    SSE event is not significant. In actuality, the amount of secondary-
    to-primary leakage in the event of a LOCA + SSE is expected to be 
    less than that originally allowed, i.e., 500 gpd per steam 
    generator. Furthermore, secondary-to-primary in-leakage would be 
    less than primary-to-secondary leakage for the same pressure 
    differential since the cracks would tend to tighten under a 
    secondary-to-primary pressure differential. Also, the presence of 
    the tube support plate is expected to reduce the amount of in-
    leakage.
        Addressing the R.G. 1.83 considerations, implementation of the 
    tube repair criteria is supplemented by 100% inspection requirements 
    at the tube support plate elevations having outside diameter stress 
    corrosion cracking indications, reduced operating leakage limits, 
    eddy current inspection guidelines to provide consistency in voltage 
    normalization, and rotating probe inspection requirements for the 
    larger indications left in service to characterize the principle 
    degradation mechanism as outside diameter stress corrosion cracking.
        As noted previously, implementation of the tube support plate 
    elevation repair criteria will decrease the number of tubes that 
    must be taken out of service with tube plugs or repaired. The 
    installation of steam generator tube plugs or tube sleeves would 
    reduce the RCS flow margin, thus implementation of the voltage-based 
    repair criteria will maintain the margin of flow that would 
    otherwise be reduced through increased tube plugging or sleeving.
        Considering the above, it is concluded that the proposed change 
    does not result in a significant reduction in margin with respect to 
    plant safety as defined in the Final Safety Analysis Report or any 
    bases of the plant Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: Herbert N. Berkow
    
    Southern Nuclear Operating Company, Inc., Docket No. 50-364, Joseph 
    M. Farley Nuclear Plant, Unit 2, Houston County, Alabama
    
        Date of amendment request: April 22, 1996
        Description of amendment request: The proposed amendment would 
    implement a new F* criterion based on maintaining existing safety 
    margins for steam generator tube structural integrity concurrent with 
    allowance for NDE (nondestructive examination) eddy current 
    uncertainty.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The proposed change retains the existing margin in the F* 
    distance used to meet regulatory guidance of draft Regulatory Guide 
    1.121 and only changes the amount of assumed NDE eddy current 
    uncertainty based on the type of eddy current technology utilized in 
    the inspection. Therefore, there is no significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated. WCAP 
    11306, Revision 2, ``Tubesheet Region Plugging Criterion for the 
    Alabama Power Company Farley Nuclear Station Unit 2 Steam 
    Generators,'' provides adequate basis for the F* distance proposed 
    of 1.54 plus allowance for eddy current uncertainty measurement. 
    Since the value of 1.54 inches was used in the analysis no new or 
    different kind of accident from any accident previously evaluated 
    will be created.
        3. The proposed change does not involve a significant reduction 
    in a margin safety. Since the value of 1.54 inches already is used 
    in the steam generator tube pull out analysis, there is no 
    significant change to a margin safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: Herbert N. Berkow
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, MissouriDate of application request: February 23, 
    1996, as supplemented by letter dated April 24, 1996.
    
        Description of amendment request: The amendment would add a 
    footnote in the license for Callaway Plant, Unit No. 1 to indicate that 
    Union Electric Company has entered into a merger agreement with CIPSCO 
    Incorporated which provides for Union Electric Company to become a 
    wholly-owned operating company of Ameren Corporation, a registered 
    public utility holding company under the Public Utility Holding Company 
    Act of 1935, as amended. After the merger, Union Electric Company would 
    continue to own and operate the Callaway Plant as an operating company 
    subsidiary of Ameren Corporation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change does not affect accident initiators or 
    assumptions. The radiological consequences of any accident 
    previously evaluated remain unchanged. The change is an 
    administrative change to reflect Union Electric's status as an 
    operating company subsidiary of Ameren.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not reduce the margin of safety assumed 
    in any accident analysis or affect any safety limits. The change is 
    administrative and reflects Union Electric's status as an operating 
    company subsidiary of Ameren.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not reduce the margin of safety assumed 
    in any accident
    
    [[Page 25714]]
    
    analysis or affect any safety limits. The change is administrative 
    and reflects Union Electric's status as an operating company 
    subsidiary of Ameren.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: April 30, 1996
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    3.1.b.1, its associated bases, and Figure TS 3.1-4 by extending the low 
    temperature overpressure protection (LTOP) requirements through the end 
    of operating cycle 33 or 33.41 effective full power years. The only 
    technical change being proposed is the substitution of end of life 
    fluence for the end of operating cycle 21 fluence.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change was reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed change will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The LTOP setpoint and revised P/T [pressure/temperature] limits 
    reflected in proposed Figure TS 3.1-4 ensure that the Appendix G 
    pressure/temperature limits are not exceeded, and therefore, help 
    ensure that RCS integrity is maintained. The changes do not modify 
    the reactor coolant system pressure boundary, nor make any physical 
    changes to the facility design, material, construction standards, or 
    setpoints. The LTOP valve setpoint remains set at 500 psi. The LTOP 
    enabling temperature based on Figure TS 3.1-2 is 338 deg.F and is 
    more conservative than a value of 303 deg. Figure TS 3.1-4. The LTOP 
    enabling temperature based on Figure TS 3.1-2 remains unchanged by 
    this PA [proposed amendment]. The probability of a LTOP event 
    occurring is independent of the pressure-temperature limits for the 
    RCS pressure boundary. Therefore, the probability of a LTOP event 
    occurring remains unchanged.
        The calculation of pressure temperature limits in accordance 
    with approved regulatory methods provides assurance that reactor 
    pressure vessel fracture toughness requirements are met and the 
    integrity of the RCS [reactor coolant system] pressure boundary is 
    maintained. Similar methodology was used in calculations to support 
    approved amendment 120 to the Kewaunee Technical Specifications 
    dated April 26, 1995. The material property basis, including 
    chemistry factor and initial reference temperature for the 
    unirradiated material (RTNDT), used for this PA is the same as 
    that used in the current TS. The only technical change being made in 
    this PA is the use of end of life fluence.
        The use of predicted fluence values through the end of operating 
    cycle 33 is appropriately considered within the calculations in 
    accordance with standard industry methodology previously docketed 
    under WCAP 13227 and WCAP 14279. The neutron exposure projections 
    utilized for calculation of the reference temperature were 
    multiplied by a factor of 1.11 to adjust for biases observed between 
    cycle specific calculations and the results of neutron dosimetry for 
    the four surveillance capsules removed from the KNPP reactor. The 
    factor of 1.11 was derived by taking the average of the measured to 
    calculation (M/C) flux ratios obtained from the dosimetry results of 
    capsules V, R, P, and S removed from the KNPP reactor vessel. The 
    resulting effect of using predicted fluence values through the end 
    of cycle 33 instead of cycle 21 is to require the plant to evaluate 
    LTOP transients to more limiting requirements. The proposed PT 
    limits are shifted to a lower pressure and higher temperature, which 
    is more conservative.
        The changes do not adversely affect the integrity of the RCS 
    such that its function in the control of radiological consequences 
    is affected. In addition, the changes do not affect any fission 
    barrier. The changes do not degrade or prevent the response of the 
    LTOP relief valve or other safety related system to accidents 
    described in Chapter 14 of the USAR. In addition, the changes do not 
    alter any assumption previously made in the radiological 
    consequences evaluations nor affect the mitigation of the 
    radiological consequences of an accident described in the USAR. 
    Therefore, the consequences of an accident previously evaluated in 
    the USAR will not be increased.
        Thus, the operation of KNPP Unit 1 in accordance with the PA 
    does not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. Create the possibility of a new or different type of accident 
    from an accident previously evaluated.
        The Appendix G pressure temperature limitations were prepared 
    using methods derived from the ASME Boiler and Pressure Vessel Code 
    and the criteria set forth in NRC Regulatory Standard Review Plan 
    5.3.2. The changes do not cause the initiation of any accident nor 
    create any new credible limiting failure for safety-related systems 
    and components. The changes do not result in any event previously 
    deemed incredible being made credible. As such, it does not create 
    the possibility of an accident different than any evaluated in the 
    USAR.
        The changes do not have any effect on the ability of the safety-
    related systems to perform their intended safety functions. The 
    changes do not create failure modes that could adversely impact 
    safety-related equipment. Therefore, it will not create the 
    possibility of a malfunction of equipment important to safety 
    different than previously evaluated in the USAR. Thus, the PA does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The use of Paragraph (c)(2)(ii)(A) of 10 CFR 50.61, initial 
    reference temperature of -50 deg.F, and the fluence values through 
    EOC [end of cycle] 33 does not modify the reactor coolant system 
    pressure boundary, nor make any physical changes to the LTOP 
    setpoint or system design. Proposed Figure TS 3.1-4 was prepared in 
    accordance with regulatory requirements and requires evaluation of 
    LTOP events to more limiting requirements of neutron exposure 
    projections of 33.41 EFPY instead of 18.40 EFPY.
        Therefore, the PA does not create the possibility of a new or 
    different type of accident from any accident previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        The Appendix G pressure temperature limitations were prepared 
    using methods derived from the ASME Boiler and Pressure Vessel Code 
    and the criteria set forth in NRC Regulatory Standard Review Plan 
    5.3.2. These documents along with the calculational limitations 
    specified in 10 CFR 50.61 are an acceptable method for implementing 
    the requirements of 10 CFR 50 Appendices G and H. Inherent 
    conservatism in the P/T limits resulting from these documents 
    include:
        a. An assumed defect in the reactor vessel wall with a depth 
    equal to 1/4 of the thickness of the vessel wall (1/4T) and a length 
    equal to 1-1/2 times the thickness of the vessel wall.
        b. Assumed reference flaw oriented in both longitudinal and 
    circumferential directions and limiting material property. At KNPP, 
    the only weld in the core region is oriented in the circumferential 
    direction.
        c. A factor of safety of 2 is applied to the membrane stress 
    intensity factor.
        d. The limiting toughness is based upon a reference value 
    (KIR) which is a lower bound on the dynamic crack initiation or 
    arrest toughness.
        e. A 2-sigma margin term is applied in determining the adjusted 
    reference temperature (ART) that is used to calculate the limiting 
    toughness.
        Similar methodology was used in calculations to support approved 
    amendment 120 dated April 26, 1995. Beyond the conservatism 
    described above, WPSC
    
    [[Page 25715]]
    
    [Wisconsin Public Service Corporation] has incorporated the 
    following additional margin in preparing this PA:
        a. The neutron exposure projections were multiplied by a factor 
    of 1.11 to adjust for biases observed between cycle specific 
    calculations and the results of neutron dosimetry for the four 
    surveillance capsules removed from the KNPP reactor. The factor of 
    1.11 was derived by taking the average of the measured to 
    calculation (M/C) flux ratios obtained from the dosimetry results of 
    capsules V, R, P, and S removed from the KNPP reactor vessel.
        b. The calculated material-specific chemistry factor value is 
    191.27 and is based on KNPP surveillance capsule data from capsules 
    V, R, and P. Utilization of KNPP's most recent surveillance capsule 
    data from capsule S results in chemistry factor value of 190.6. 
    Consistent with calculation C10689, Revision 1 the value used for 
    chemistry factor in this PA remains 191.27, which is conservative.
        c. The LTOP enabling temperature based on Figure TS 3.1-2 is 
    338 deg.F and is more conservative than a value of 303 deg.F which 
    is supported by proposed Figure TS 3.1-4. The LTOP enabling 
    temperature based on Figure TS 3.1-2 remains unchanged by this PA.
        d. The reactor coolant pump starting restrictions of TS 
    3.1.a.1.c remain in place.
        An alternative methodology to the safety margins required by 
    Appendix G to 10 CFR Part 50 has been developed by the ASME Working 
    Group on Operating Plant Criteria. This methodology is contained in 
    ASME Code Case N-514. The Code Case N-514 provides criteria to 
    determine pressure limits during LTOP events that avoid certain 
    unnecessary operational restrictions, provide adequate margins 
    against failure of the reactor pressure vessel, and reduce the 
    potential for unnecessary activation of the relief valve used for 
    LTOP. Specifically, the ASME Code Case N-514 allows determination of 
    the setpoint for LTOP events such that the maximum pressure in the 
    vessel would not exceed 110% of the P/T limits of the existing ASME 
    Appendix G; and redefines the enabling temperature as a coolant 
    temperature less than 200 deg.F or a reactor vessel metal 
    temperature less than RTNDT + 50 deg.F greater. Code Case N-
    514, ``Low Temperature Overpressure Protection,'' has been approved 
    by the ASME Code Committee but not yet approved for use in 
    Regulatory Guide 1.147. The content of this code case has been 
    incorporated into Appendix G of Section XI of the ASME Code and 
    published in the 1993 Addenda to Section XI. It is expected that 
    when the NRC revises 10 CFR 50.55a, it will endorse the 1993 Addenda 
    and Appendix G of Section XI into the regulations. As stated above, 
    this PA utilizes Appendix G limits and an enabling temperature 
    corresponding to a reactor vessel metal temperature less than 
    RTNDT + 90 deg.F, which is more conservative than the 
    alternative methodology contained in Code Case N-514.
        The revised calculations meet the NRC acceptance criteria for 
    the LTOP setpoint and system design as described in NRC Safety 
    Evaluation Report (SER) dated September 6, 1995 which concluded that 
    ``the spectrum of postulated pressure transients would be 
    mitigated...such that the temperature pressure limits of Appendix G 
    to 10 CFR 50 are maintained.''
        Utilization of methodology set forth in the ASME Boiler and 
    Pressure Vessel Code, NRC Regulatory Standard Review Plan 5.3.2, 10 
    CFR 50.61, and 10 CFR 50 Appendices G and H with the above 
    additional margins ensures that proper limits and safety factors are 
    maintained. Thus, the PA does not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497
        NRC Project Director: Gail H. Marcus
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: May 1, 1996
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    4.2.b, ``Steam Generator Tubes,'' its associated bases, and Figure TS 
    4.2-1 by redefining the pressure boundary for Westinghouse mechanical 
    hybrid expansion joint (HEJ) steam generator (SG) tube sleeves. The 
    proposed amendment supersedes in its entirety a previously submitted 
    proposed amendment dated October 6, 1995, which was published in the 
    Federal Register on November 8, 1995 (60 FR 56372).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        This proposed change was reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist.
        1. Operation of the KNPP in accordance with the proposed license 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        Mechanical testing shows inherent structural integrity of the 
    HEJ [hybrid expansion joint] upper joint such that the tube rupture 
    capability recommendations of RG [Regulatory Guide] 1.121 are met, 
    even for instances of 100-percent throughwall, 360 degree 
    degradation in the HRLT [hardroll lower transition] region. 
    Structural test results are documented in WCAPs-14157, -14157 
    Addendum 1, -14446 and -14641. Based on this test data, the 
    structural recommendations of RG 1.121 are satisfied when there is a 
    difference of at least 0.003 inch, between the maximum hardroll 
    diameter of the sleeve, and the diameter at the elevation of the PTI 
    [parent tube indication] center line; i.e. there is an interference 
    lip of 0.003 inch or more. The proposed pressure boundary will allow 
    PTIs located such that there is a minimum diameter change of 0.003 
    inch (not including an allowance for measurement uncertainty) 
    between the maximum point of the sleeve hardroll, and the diameter 
    at the elevation of the PTI peak amplitude to remain in service. 
    Based on the high degree of structural integrity of the HEJ upper 
    joint, it can be concluded that application of the revised pressure 
    boundary criteria will not result in an increased probability of an 
    accident previously evaluated.
        Each sleeved tube with a PTI located in the HRLT such that there 
    is a change in diameter of 0.003 inch to 0.013 inch, will be 
    assigned a conservatively bounding primary-to-secondary SLB [steam 
    line break] leakage value of 0.025 gpm per indication. Indications 
    located such that there is a change in diameter of greater than 
    0.013 inch will not contribute to the SLB leakage. The total number 
    of indications remaining in service will be limited such that the 
    primary-to-secondary leakage during a postulated SLB will not exceed 
    a small fraction of the 10 CFR Part 100 guidelines. For KNPP this 
    has been calculated to be 34.0 gpm for the faulted loop. Therefore, 
    it can be concluded that application of the revised pressure 
    boundary criteria will not increase the consequences of an accident 
    previously evaluated.
        2. The proposed license amendment request does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Implementation of the revised pressure boundary will not 
    introduce a change to the design basis or operation of the plant. 
    Mechanical testing of degraded sleeve joints supports the 
    conclusions that the joint retains structural integrity (tube burst) 
    capability consistent with RG 1.121, and leakage integrity with 
    regards to a small fraction of the 10 CFR Part 100 guidelines. As 
    with the initial installation of the sleeves, implementation of the 
    relocated pressure boundary does not interact with other portions of 
    the reactor coolant system. Any hypothetical accident as a result of 
    potential PTIs is bounded by the existing tube rupture accident 
    analysis. Neither the sleeve design nor implementation of the 
    redefined pressure boundary affects any other component or location 
    of the tube outside of the immediate area repaired. Therefore 
    application of the revised pressure boundary criteria will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in the margin of safety.
    
    [[Page 25716]]
    
        The safety factors used in establishment of the HEJ sleeved tube 
    pressure boundary are consistent with the safety factors in the ASME 
    Boiler and Pressure Vessel Code used in SG [steam generator] design. 
    Based on the sleeve-to-tube geometry, it is unrealistic to consider 
    that application of the revised pressure boundary could result in 
    single tube leak rates exceeding the normal makeup capacity during 
    normal operating conditions. The pressure boundary developed in 
    WCAPs-14446 and -14641 have been developed using the methodology of 
    RG 1.121. The performance characteristics of the postulated degraded 
    parent tubes of HEJ sleeve/tube joints have been verified by testing 
    to retain structural integrity and preclude significant leakage 
    during normal and postulated accident conditions. Testing indicates 
    that postulated circumferentially separated tubes which the pressure 
    boundary [addresses] would not experience axial displacement during 
    either normal operation or SLB conditions. The existing offsite dose 
    evaluation performed for KNPP in support of the voltage based repair 
    criteria for axial ODSCC [outside diameter stress corrosion 
    cracking] at TSP [tube support plate] intersections established a 
    faulted loop primary to secondary leak rate of 34.0 gpm. Following 
    implementation of the criteria, postulated leakage from all sources 
    must not exceed 34.0 gpm in the faulted loop. Maintenance of this 
    limit will ensure that offsite doses would not exceed the currently 
    accepted limit of a small fraction of the 10 CFR Part 100 
    guidelines. The pressure boundary definition uses a conservatively 
    established ``per indication'' leak rate for estimation of SLB 
    leakage. This leak rate is applied to all indications left in 
    service within the HRLT, regardless of indications length and 
    throughwall extent. Application of the revised pressure boundary 
    criteria will not result in a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497
        NRC Project Director: Gail H. Marcus
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 29, 1994, as superseded by letter 
    dated September 15, 1995, and supplements dated March 8, 1996, and 
    April 18, 1996
        Description of amendment request: The proposed amendment revises TS 
    3/4.8.1 and its associated Bases to improve overall emergency diesel 
    generator reliability and availability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        These proposed changes do not involve a change in the 
    operational limits or physical design of the emergency power system. 
    Emergency diesel generator operability and reliability will continue 
    to be assured while minimizing the number of required emergency 
    diesel generator starts. Also, emergency diesel generator 
    reliability will be enhanced by minimizing severe test conditions 
    which can lead to premature failures.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        These proposed changes do not involve a change in the 
    operational limits or physical design of the emergency power system. 
    The performance capability of the emergency diesel generator will 
    not be affected. Emergency diesel generator reliability and 
    availability will be improved by the implementation of the proposed 
    changes. There is no actual impact on any accident analysis.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        These proposed change do not involve a change in the operational 
    limits or physical design of the emergency power system. The 
    performance capability of the emergency diesel generator will not be 
    affected. Emergency diesel generator reliability and availability 
    will be improved by the implementation of the proposed changes. No 
    margin of safety is reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: May 1, 1996
        Description of amendment request: This license amendment request 
    proposes to revise Section 6.0 of the technical specifications to 
    reflect position title changes within the Wolf Creek Nuclear Operating 
    Corporation (WCNOC) organization.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change does not involve a significant increase in 
    the probability of consequences of an accident previously evaluated. 
    These changes involve administrative changes to the WCNOC 
    organization and to the position qualification of plant personnel.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    This change is administrative in nature and does not involve a 
    change to the installed plant systems or the overall operating 
    philosophy of Wolf Creek Generating Station.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not involve a significant reduction in 
    a margin of safety. This change does not involve any changes in 
    overall organizational commitments. A position title change alone 
    does not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    [[Page 25717]]
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: April 25, 1996
        Brief description of amendment request: The amendment relocates the 
    technical specification (TS) Traversing In-Core Probe System Limiting 
    Condition for Operation 3/4.3.7.7 and its Bases 3/4.3.7.7 to the 
    Technical Requirements Manual, and modifies Note (f) of TS Table 
    4.3.1.1-1.
        Date of publication of individual notice in Federal Register: May 
    8, 1996 (61 FR 20840)
        Expiration date of individual notice: June 7, 1996
        Local Public Document Room location:  Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, OES Nuclear, 
    Inc., Pennsylvania Power Company, Toledo Edison Company, Docket No. 
    50-440, Perry Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: April 26, 1996
        Brief description of amendment request: The proposed amendment 
    would correct minor technical and administrative errors in the Improved 
    Technical Specifications prior to its implementation.
        Date of individual notice in Federal Register: May 9, 1996 (61 FR 
    21213)
        Expiration date of individual notice: June 10, 1996
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: February 1, 1996
        Brief description of amendments: These amendments revised (1) 
    Technical Specifications (TS) 3/4.1.1.1, 6.9.1.9, and 6.9.1.10 to 
    relocate the shutdown margin (reactor trip breakers open) to the Core 
    Operating Limits Report; (2) TS 3/4.3.2 (Tables 3.3-3 and 3.3-4) to 
    specify an additional restriction for the allowed low-pressurizer-
    pressure trip setpoint when reducing reactor coolant (RCS) system 
    pressure in Mode 3; (3) TS Section 2.2.1 (Table 2.2-1) to make it 
    consistent with the footnote in TS Tables 3.3-3 and 3.3-4; and (4) TS 
    Sections 3/4.5.2 and 3/4.5.3 to require two emergency core cooling 
    system subsystems to be operable in Mode 3 whenever the RCS cold-leg 
    temperature is equal to or above 485 deg.F. The Table of Contents and 
    the Bases are also revised to reflect these changes.
        Date of issuance: April 30, 1996
        Effective date: April 30, 1996, to be implemented within 45 days of 
    issuance
        Amendment Nos.:  Unit 1 - 106; Unit 2 - 98; Unit 3 - 78
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: March 27, 1996 (61 FR 
    13522) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 30, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: December 27, 1995
        Brief description of amendments: These amendments modify Tables 
    3.3-11 and 4.3-7 of Beaver Valley Power Station, Unit Nos. 1 and 2 
    (BVPS-1 and BVPS-2) Technical Specification 3.3.3.8 (Accident 
    Monitoring Instrumentation) such that only one valve position 
    indication system for the power-operated relief valves and safety 
    valves is required to be operable. Minor editorial changes to BVPS-1 TS 
    3.3.3.8 and its associated Action Statements are also being made. These 
    changes make the requirements of TS 3.3.3.8 consistent with the NRC's 
    Improved Standard Technical Specifications (NUREG-1431, Revision 1) and 
    with the guidance of Regulatory Guide 1.97, NUREG-0578, and NUREG-0737.
        Date of issuance: May 1, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos.: 199 and 81
    
    [[Page 25718]]
    
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3499) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 1, 1996No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley 
    Power Station, Unit No. 1, Shippingport, Pennsylvania
    
        Date of application for amendment: February 12, 1996
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 4.6.2.2.d to delete the reference to the specific 
    test acceptance criteria for the Containment Recirculation Spray Pumps 
    and replaces the specific test acceptance criteria with reference to 
    the requirements of the Inservice Testing (IST) Program. In addition, 
    the 18-month test frequency is replaced with the test frequency 
    requirements specified in the IST Program. The amendment also revises 
    the Bases for TS 4.6.2.2.d to describe this revision to TS 4.6.2.2.d.
        Date of issuance: May 7, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No: 200
        Facility Operating License No. DPR-66. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 13, 1996 (61 FR 
    10393) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 7, 1996 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida
    
        Date of application for amendments: March 21, 1996 as supplemented 
    April 8, 15, and 18, 1996.
        Description of amendment request: The proposed amendment provides 
    for interim repair criteria for volumetric intergranular attack (IGA) 
    indications in the once-through-steam generators (OTSG). The interim 
    repair criteria is based on bobbin coil voltage response and motorized 
    rotating pancake coil probe dimensional measurements. The amendment 
    would be applicable for IGA indications within the region below the 
    first tube support plate and the secondary face of the lower tubesheet 
    (first span) of the OTSG and for one cycle only until Refuel 11.
        Date of issuance: April 30, 1996
        Effective date: April 30, 1996Amendment Nos. 154
        Facility Operating License No. DPR-72: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes (61 FR 13888). That notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by April 29, 1996, but indicated that if the Commission makes a 
    final no significant hazards consideration determination any such 
    hearing would take place after issuance of amendment. The Commission's 
    related evaluation of this amendment is contained in a Safety 
    Evaluation dated April 30, 1996
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629
    
    Indiana Michigan Power Company, Docket No. 50-316, Donald C. Cook, 
    Nuclear Plant, Unit No. 2, Berrien County, Michigan
    
        Date of application for amendment: March 12, 1996 (AEP:NRC:1248)
        Brief description of amendment: The amendment removes the technical 
    specifications related to shutdown and control rod position indication 
    while in shutdown modes 3, 4, and 5.
        Date of issuance: May 2, 1996
        Effective date: May 2, 1996, with full implementation within 45 
    days
        Amendment No.: 194
        Facility Operating License No. DPR-74. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 27, 1996 (61 FR 
    13527) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 2, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
    
    Nebraska Public Power District, Docket No. 50-298, Cooper Nuclear 
    Station, Nemaha County, Nebraska
    
        Date of amendment request: May 5, 1995 and July 14, 1995, 
    supplemented by letter dated March 5, 1996
        Brief description of amendment: The amendment revised the Technical 
    Specifications to 1) verify that the redundant diesel generator is 
    operable upon the loss of one diesel generator, and implement 
    provisions to verify that the operable diesel generator does not have a 
    common cause failure; 2) incorporate provisions to allow a modified 
    start for the diesel generators; and 3) remove the requirement that the 
    reactor power level be reduced to 25% of rated power upon loss of both 
    diesel generator units or both incoming power sources (start-up and 
    emergency transformers). In addition, the period of time allowed for 
    continued reactor operation with both diesels inoperable was reduced 
    from 24 to two hours.
        Date of issuance: April 29, 1996
        Effective date: April 29, 1996
        Amendment No.: 175
        Facility Operating License No. DPR-46: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49939) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 29, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Auburn Memorial Library, 1810 
    Courthouse Avenue, Auburn, NE 68305.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: September 22, 1995
        Description of amendment request: The amendment changes the ACTION 
    specified in Table 3.3-3, Engineered Safety Features Actuation System 
    Instrumentation, from ACTION 18 to ACTION 15 for Functional Unit 8.b, 
    Automatic Switchover to Containment Sump - RWST Level Low-Low.
        Date of issuance: May 7, 1996,
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 47
        Facility Operating License No. NPF-86. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62493) The Commission's related
    
    [[Page 25719]]
    
    evaluation of the amendment is contained in a Safety Evaluation dated 
    May 7, 1996. No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: May 26, 1995, as supplemented 
    October 20, 1995, and May 3, 1996.
        Brief description of amendment: The amendment modifies Technical 
    Specification (TS) 3.8.1.2, ``Electrical Power Systems, Shutdown,'' TS 
    3.8.2.2, ``Electrical Power Systems, A.C. Distribution - Shutdown,'' 
    and TS 3.8.2.4, ``Electrical Power Systems, D.C. Distribution - 
    Shutdown,'' to provide operational flexibility as well as consistency 
    between action statements and to eliminate certain surveillance 
    requirements that are not applicable in Mode 5 or 6.
        The proposed changes relating to TS 3.8.1.1, ``Electrical Power 
    Systems, A.C. Sources, Operating,'' are not included in this amendment 
    since this portion of the TS change is still under review by the staff 
    and will be addressed at a later date.
        Date of issuance: May 6, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 197
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 6, 1995 (60 FR 
    62493) The October 20, 1995, letter formally withdrew the need for 
    exigent handling of the May 26, 1995, request and requested an 
    additional change to TS 3.8.2.4. The May 3, 1996, letter withdrew a 
    portion of the initial request which did not affect the initial 
    proposed no significant hazards consideration. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    May 6, 1996. No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT 06385.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment:  March 14, 1996
        Brief description of amendment: The amendment allows a one-time 
    extension of the intervals for the pressurizer safety valve setpoint 
    and snubber functional testing that is due in May 1996.
        Date of issuance: May 3, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 165
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 3, 1996, (61 FR 
    14835) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 3, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: January 4, 1996
        Brief description of amendments: The amendments change Technical 
    Specification 3/4.8.2.5, ``28-Volt D.C. Distribution - Operating.'' The 
    amendment for Unit 1 makes Unit 1 requirements similar to Unit 2 by 
    defining the specific battery chargers that are required for each train 
    and by restricting the use of the backup battery charger to 7 days. The 
    amendments for both units also require that the 28-Volt DC bus be 
    energized for that bus to be OPERABLE.
        Date of issuance: April 29, 1996
        Effective date: Both units, as of date of issuance, to be 
    implemented within 60 days.Amendment Nos. 182 and 163
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5818) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 29, 1996No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: September 6, 1995, as 
    supplemented by letters dated January 30, 1996, March 27, 1996, and 
    April 2, 1996.
        Brief description of amendment: The amendment revises TS 5.3.1 to 
    reflect a change in the maximum initial enrichment for reload fuel, 
    subject to the integral fuel burnable absorber (IFBA) requirements, and 
    a change in the maximum fuel enrichment not requiring IFBAs. The 
    amendment also changes the maximum reference kinfinity in TS 
    5.6.1.1 for fuel storage in Region 1 of the spent fuel pool and revises 
    TS Figure 3.9-1 to reflect a change to the maximum initial enrichment 
    for fuel stored in Region 2 of the spent fuel pool.
        Date of issuance: April 30, 1996
        Effective date: April 30, 1996, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 109
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 8, 1995 (60 FR 
    56372). The January 30, 1996, March 27, 1996, and April 2, 1996, 
    supplemental letters provided additional clarifying information and did 
    not change the original no significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 30, 1996.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: February 9, 1996
        Brief description of amendment: The amendment revised Technical 
    Specification 5.3.1 to allow the use of ZIRLO clad fuel rods and ZIRLO 
    filler rods.
        Date of issuance: April 30, 1996
        Effective date: April 30, 1996, to be implemented within 30 days of 
    issuance.
        Amendment No.: 110
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7558) The Commission's related
    
    [[Page 25720]]
    
    evaluation of the amendment is contained in a Safety Evaluation dated 
    April 30, 1996.No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
    
        Date of application for amendments: January 30, 1996
        Brief description of amendments: These amendments modify the 
    Technical Specifications requirements for the sampling of the reactor 
    coolant for dissolved oxygen chlorides and fluorides.
        Date of issuance: 209 and 209
        Effective date: April 29, 1996
        Amendment Nos. 209 and 209
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 27, 1996 (61 FR 
    13533) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 29, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: January 19, 1996, as 
    supplemented by letter dated March 19, 1996.
        Brief description of amendment: The amendment modifies the 
    Technical Specifications for leak tests of containment isolation 
    valves. The amendment replaces the current specified surveillance 
    intervals for containment leak testing with new surveillance 
    requirements to conduct containment leak testing according to a 
    performance-based containment leak test program.
        Date of issuance: May 8, 1996
        Effective date: May 8, 1996, to be implemented within 30 days of 
    issuance.
        Amendment No.: 144
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5820) The March 19, 1996, supplemental letter provided additional 
    clarifying information and did not change the initial no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    May 8, 1996.No significant hazards consideration comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Dated at Rockville, Maryland, this 15th day of May 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation
    [Doc. 96-12691 Filed 5-21-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
05/22/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-20522
Dates:
April 30, 1996, to be implemented within 45 days of issuance
Pages:
25696-25720 (25 pages)
PDF File:
x96-20522.pdf