97-11910. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 146 (Wednesday, July 30, 1997)]
    [Notices]
    [Pages 40843-40868]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-11910]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
    
    [[Page 40844]]
    
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from July 3, 1997, through July 18, 1997. The 
    last biweekly notice was published on July 16, 1997.
    
    Notice of Consideration of Issuance of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By August 29, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with
    
    [[Page 40845]]
    
    the Secretary of the Commission, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, Attention: Docketing and Services Branch, or 
    may be delivered to the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington DC, by the above date. A copy 
    of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendments request: May 23, 1997
        Description of amendments request: The proposed amendment would 
    revise Technical Specification 3/4.4.4 to allow the installation of 
    ABB/CE welded sleeves, in accordance with ABB/CE Topical Report CEN-
    630-P, ``Repair of 3/4 Inch Outer Diameter Steam Generator Tubes Using 
    Leak Tight Sleeves,'' Revision 1, in the Palo Verde Units 1, 2 and 3 
    steam generators.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below: 1. The proposed change does 
    not involve a significant increase in the probability or consequences 
    of an accident previously evaluated.
        The proposed amendment to permit the use of steam generator tube 
    sleeves as an alternative to tube plugging is a safe and effective 
    repair procedure that does not result in removing a tube from 
    service. Mechanical strength, corrosion resistance, installation 
    methods, and inservice inspection techniques of sleeves have been 
    shown to meet NRC acceptance criteria.
        Analytical verifications were performed using design and 
    operating transient parameters selected to envelope loads imposed 
    during normal operating and accident conditions. Fatigue and stress 
    analysis of sleeved tube assemblies were completed in accordance 
    with the requirements of Section III of the ASME Code. The results 
    of qualification testing, analysis and plant operating experience at 
    other facilities demonstrates that the sleeving process is an 
    acceptable means of maintaining steam generator tube integrity. The 
    sleeve configuration has been designed and analyzed in accordance 
    with the structural margins specified in Regulatory Guide 1.121 (RG 
    1.121). Furthermore, the installed sleeve will be monitored through 
    periodic inspections on a sample basis with eddy current techniques. 
    A sleeve-specific plugging margin, per the recommendations of 
    Regulatory Guide 1.121, has been specified with appropriate 
    allowances for NDE uncertainty and defect growth rate. Therefore, 
    since the sleeve provides the same protection against a tube rupture 
    as the original tube, the use of sleeves does not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        Recently, industry experience with forced shutdown events 
    associated with tube failures at sleeve junctions was assessed by 
    APS and ABB-CE. The root cause of these events has been attributed 
    to the lack of proper post-installation stress relief and/or the 
    imposition of high stresses due to tube growth restrictions at 
    locked tube supports. The material and design of the PVNGS steam 
    generator supports minimizes the potential for locked supports. The 
    tube supports are of eggcrate design and are constructed of ferric 
    stainless steel. The large flow area in the eggcrate design provides 
    better irrigation and reduces the potential for steam blanketing, 
    therefore, the tube-to-tube support crevices are less likely to be 
    blocked by crud, boiler water deposits and corrosion products. Since 
    the support material is type 409 ferric stainless steel, it is not 
    susceptible to magnetite corrosion which has resulted in denting and 
    lockup at plants with carbon steel supports. These conclusions have 
    been substantiated via tube pull activities conducted in PVNGS Unit 
    2. Although ABB/CE does not require post-weld heat treatment in all 
    applications, APS will require that a post-weld stress relief be 
    conducted for sleeve installations. Therefore, with proper sleeve 
    installation the proposed change will not involve a significant 
    increase in the probability of an accident previously evaluated.
        The consequences of accidents previously analyzed are not 
    increased as a result of sleeving activities. The hypothetical 
    failure of the sleeve would be bounded by the current steam 
    generator tube rupture analysis contained in the PVNGS UFSAR. Due to 
    the slight reduction in diameter caused by the sleeve wall 
    thickness, it is expected that the primary release rates would be 
    less than assumed for the steam generator tube rupture analysis, 
    and, therefore, would result in lower primary fluid mass release to 
    the secondary system. Additionally, further conservatism is 
    introduced if the break were postulated to occur at a location on 
    the tube higher than the location where a sleeve is installed. The 
    overall effect would be reduced steam generator tube rupture release 
    rates. The minimal reduction in flow area associated with a tube 
    sleeve has no significant affect on steam generator performance with 
    respect to heat transfer or system flow resistance and pressure 
    drop. The installation of sleeves rather than plugging also 
    maintains a greater heat transfer surface in the steam generator. In 
    any case, the impacts are bounded by evaluations which demonstrate 
    the acceptability of tube plugging, which totally removes the tube 
    from service.
        Therefore, in comparison to plugging, tube sleeving is 
    considered a significant improvement with respect to steam generator 
    performance. Therefore, based on the above, the proposed amendment 
    does not significantly increase the probability or consequences of 
    an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        A sleeved steam generator tube performs the same function in the 
    same passive manner as an unsleeved steam generator tube. Tube 
    sleeves are designed and qualified to the stress and pressure limits 
    of Section III of the ASME Code and Regulatory Guide 1.121.
        The installation of the sleeve, including weld and welder 
    qualification and nondestructive examination (NDE), meets or exceeds 
    the requirements of ASME Section XI. Three types of NDE are 
    conducted. Ultrasonic Testing (UT) is performed to verify the 
    adequacy of the tube to sleeve weld assuring proper fusion. Eddy 
    Current testing (ECT) is performed following each installation to 
    establish baseline data for each sleeve in order to monitor future 
    degradation of the primary to secondary pressure boundary. Visual 
    inspections will be performed to verify or ascertain the mechanical 
    and structural condition of a weld. Critical conditions which are 
    checked include weld width and completeness, and the absence of 
    visibly noticeable indications such as cracks, pits, and burn 
    through.
        ABB Combustion Engineering, Inc., Report CEN-630-P, Revision 01, 
    ``Repair of 3/4'' O.D. Steam Generator Tubes Using Leak Tight 
    Sleeves'' dated November, 1996, demonstrates that the repair of 
    degraded steam generator tubes using tube sleeves will result in 
    tube bundle integrity consistent with the original design basis. 
    Extensive analyses and testing have been performed on the sleeve and 
    sleeve to tube joints to demonstrate that the design criteria are 
    met. The proposed amendments have no significant effect on the 
    configuration of the plant, and the change does not affect the way 
    in which the plant is operated. Therefore, reactor operation with 
    sleeves installed in the steam generator tubes does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
    
    [[Page 40846]]
    
        Evaluation of the sleeved tubes indicates no detrimental effects 
    on the sleeve-tube assembly resulting from reactor coolant system 
    flow, coolant chemistries, or thermal and pressure conditions. 
    Structural analyses have been performed for sleeves which span the 
    tube at the top of the tube sheet and which span the flow 
    distribution plate or eggcrate support. Mechanical testing has been 
    performed to support the analyses. Corrosion testing of typical 
    sleeve-tube assemblies has been completed and reveals no evidence of 
    sleeve or tube corrosion considered detrimental under anticipated 
    service conditions.
        Steam generator tube integrity is maintained under the same 
    limits for sleeved tubes as for unsleeved tubes, ie., Section III of 
    the ASME Code and Regulatory Guide 1.121. The portions of the 
    installed sleeve assembly which represents the reactor coolant 
    pressure boundary can be monitored for the initiation and 
    progression of sleeve/tube wall degradation, thus satisfying the 
    requirements of Regulatory Guide 1.83. The degradation limit at 
    which a sleeve/tube boundary is considered inoperable has been 
    analyzed in accordance with Regulatory Guide 1.121 and is specified 
    in the proposed amendment. Eddy current detectability of flaws has 
    been verified by ABB Combustion Engineering. Additionally, the 
    Technical Specifications continue to require monitoring and 
    restriction of primary- to- secondary system leakage through the 
    steam generators. The minimal reduction in RCS flow due to sleeving 
    results in an insignificant impact on RCS operation during normal or 
    accident conditions and is bounded by tube plugging evaluations.
        Based upon the testing and analyses performed, the installation 
    of tube sleeves will not result in a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: 3April 30, 1997
        Description of amendments request: The proposed amendments would 
    revise Surveillance Requirements (SRs) 4.7.2.b.2 and 4.7.2.c in the 
    Technical Specifications for the Brunswick Steam Electric Plant, Units 
    1 and 2. These SRs require periodic testing of the control room 
    emergency ventilation system charcoal filters. The proposed amendments 
    would revise the temperature and relative humidity conditions under 
    which the testing is performed. The revised conditions were selected to 
    approximate operating or accident conditions. Testing at the revised 
    conditions is more conservative than testing at the currently required 
    conditions. Additionally, the proposed amendments would relax the 
    acceptance criterion for filtration efficiency from 95% to a value 
    corresponding to a filtration efficiency of 90%. The 90% value is the 
    filtration efficiency assumed in the current bounding calculations for 
    control room dose under accident conditions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendments do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed amendments revise Surveillance Requirements 
    4.7.2.b.2 and 4.7.2.c to require testing of the control room
        emergency ventilation system (CREVS) charcoal in accordance with 
    ASTM D3803-1989, ``Standard Test Method for Nuclear-Grade Activated 
    Carbon.'' Currently, Surveillance Requirements 4.7.2.b.2 and 4.7.2.c 
    to [sic] require testing in accordance with the criteria of 
    Regulatory Position C.6.a of Regulatory Guide 1.52, Revision 1, 
    1976. The purpose of the CREVS is to mitigate an accident. It is not 
    associated with any initiating events and, therefore, cannot affect 
    the probability of any accident.
        ASTM D3803-1989 is an industry accepted standard for charcoal 
    filter testing. The conditions employed by this standard were 
    selected to approximate operating or accident conditions of a 
    nuclear reactor which would severely reduce the performance of 
    activated carbons. The ASTM D3803-1989 testing is more stringent 
    than that required by the criteria of Regulatory Position C.6.a of 
    Regulatory Guide 1.52, Revision 1, 1976. Specifically, the testing 
    temperature of ASTM D3803-1989 is 30.0 [plus or minus] 0.2 deg.C 
    versus 80 deg.C for the Regulatory Guide 1.52 testing. Also, ASTM 
    D3803-1989 requires a relative humidity of 93 to 96% versus [greater 
    than or equal to] 70% for the Regulatory Guide 1.52 testing. Both 
    these parameters result in the ASTM D3803-1989 test being a more 
    conservative test [than] that required by the criteria of Regulatory 
    Position C.6.a of Regulatory Guide 1.52, Revision 1, 1976.
        The proposed changes to Surveillance Requirements 4.7.2.b.2 and 
    4.7.2.c require that charcoal samples tested in accordance with the 
    methodology of ASTM D3803-1989 meet the acceptance criteria of < 5.0%="" penetration="" of="" methyl="" iodide.="" this="" corresponds="" to="" a="" 90%="" filtration="" efficiency="" which="" is="" the="" filtration="" efficiency="" assumed="" in="" the="" current="" bounding="" calculations="" of="" control="" room="" doses.="" as="" such,="" the="" proposed="" acceptance="" criteria="" of="">< 5.0%="" penetration="" of="" methyl="" iodide="" ensures="" that="" general="" design="" criterion="" 19="" dose="" limits="" for="" control="" room="" operators="" are="" not="" exceeded.="" therefore,="" the="" proposed="" amendments="" do="" not="" involve="" an="" increase="" in="" the="" consequences="" of="" an="" accident.="" 2.="" the="" proposed="" amendments="" would="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" as="" stated="" above,="" the="" proposed="" amendments="" revise="" the="" required="" testing="" methodology="" for="" the="" crevs="" charcoal.="" the="" crevs="" is="" not="" associated="" with="" any="" initiating="" events.="" the="" system="" design="" is="" not="" affected="" by="" the="" proposed="" change.="" therefore,="" the="" proposed="" amendments="" cannot="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" 3.="" the="" proposed="" license="" amendments="" do="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" proposed="" amendments="" upgrade="" the="" crevs="" charcoal="" testing="" requirements="" from="" the="" criteria="" of="" regulatory="" position="" c.6.a="" of="" regulatory="" guide="" 1.52,="" revision="" 1,="" 1976="" to="" astm="" d3803-1989.="" the="" conditions="" employed="" by="" astm="" d3803-1989="" were="" selected="" to="" approximate="" operating="" or="" accident="" conditions="" of="" a="" nuclear="" reactor="" which="" would="" severely="" reduce="" the="" performance="" of="" activated="" carbons.="" the="" astm="" d3803-1989="" testing="" is="" more="" stringent="" than="" that="" required="" by="" the="" criteria="" of="" regulatory="" position="" c.6.a="" of="" regulatory="" guide="" 1.52,="" revision="" 1,="" 1976.="" the="" testing="" temperature="" of="" astm="" d3803-1989="" [is]="" lower="" than="" that="" of="" regulatory="" guide="" 1.52="" and="" the="" relative="" humidity="" required="" by="" astm="" d3803-1989="" is="" higher="" than="" that="" required="" by="" regulatory="" guide="" 1.52.="" this="" makes="" the="" astm="" d3803-1989="" test="" being="" [sic]="" a="" more="" conservative="" test="" [than]="" that="" required="" by="" the="" criteria="" of="" regulatory="" position="" c.6.a="" of="" regulatory="" guide="" 1.52,="" revision="" 1,="" 1976.="" additionally,="" the="" proposed="" acceptance="" criteria="" of="">< 5.0%="" penetration="" of="" methyl="" iodide="" ensures="" that="" general="" design="" criterion="" 19="" dose="" limits="" for="" control="" room="" operators="" are="" not="" exceeded.="" as="" such,="" the="" proposed="" license="" amendments="" do="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" university="" of="" north="" carolina="" at="" wilmington,="" william="" madison="" randall="" library,="" 601="" s.="" college="" road,="" [[page="" 40847]]="" wilmington,="" north="" carolina="" 28403-3297.="" attorney="" for="" licensee:="" william="" d.="" johnson,="" vice="" president="" and="" senior="" counsel,="" carolina="" power="" &="" light="" company,="" post="" office="" box="" 1551,="" raleigh,="" north="" carolina="" 27602="" nrc="" project="" director:="" gordon="" e.="" edison,="" acting="" carolina="" power="" &="" light="" company,="" et="" al.,="" docket="" nos.="" 50-325="" and="" 50-="" 324,="" brunswick="" steam="" electric="" plant,="" units="" 1="" and="" 2,="" brunswick="" county,="" north="" carolina="" date="" of="" amendments="" request:="" may="" 23,="" 1997="" description="" of="" amendments="" request:="" the="" proposed="" amendments="" to="" technical="" specification="" 3/4.4.5="" for="" the="" brunswick="" steam="" electric="" plant,="" units="" 1="" and="" 2,="" reduce="" the="" short-term="" limit="" for="" dose="" equivalent="" i-131="" activity="" in="" the="" reactor="" coolant="" from="" 4.0="" microcuries/gram="" to="" 3.0="" microcuries/gram.="" with="" coolant="" specific="" activity="" greater="" than="" 0.2="" microcuries/gram="" dose="" equivalent="" i-131="" but="" less="" than="" or="" equal="" to="" the="" short-term="" limit,="" operation="" of="" the="" affected="" unit="" may="" continue="" for="" up="" to="" 48="" hours="" provided="" that="" operation="" under="" these="" conditions="" does="" not="" exceed="" 10="" percent="" of="" the="" unit's="" total="" yearly="" operating="" time.="" with="" coolant="" specific="" activity="" greater="" than="" 0.2="" microcuries/gram="" i-131="" dose="" equivalent="" for="" more="" than="" 48="" hours="" during="" one="" continuous="" time="" interval="" or="" greater="" than="" the="" short-term="" limit,="" the="" affected="" unit="" must="" be="" placed="" in="" hot="" shutdown="" within="" 12="" hours.="" the="" purpose="" of="" the="" reduction="" of="" the="" short-term="" limit="" is="" to="" ensure="" control="" room="" operator="" dose="" following="" a="" main="" steam="" line="" break="" event="" is="" within="" the="" guidelines="" contained="" in="" 10="" cfr="" part="" 100="" and="" the="" limits="" contained="" in="" criterion="" 19="" of="" appendix="" a="" to="" 10="" cfr="" part="" 50.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" 1.="" the="" proposed="" amendments="" do="" not="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" the="" proposed="" amendments="" conservatively="" revise="" action="" statements="" a.1="" and="" a.2="" of="" technical="" specification="" 3/4.4.5="" by="" reducing="" the="" maximum="" allowed="" reactor="" coolant="" specific="" activity="" from="" 4.0="" to="" 3.0="" [microcuries]/gram="" dose="" equivalent="" i-131.="" the="" purpose="" of="" the="" maximum="" allowable="" iodine="" specific="" activity="" is="" to="" ensure="" that="" the="" thyroid="" dose="" from="" a="" main="" steam="" line="" break="" (mslb="" )is="" within="" the="" 10="" cfr="" 100="" dose="" guidelines="" and="" the="" general="" design="" criteria="" 19="" dose="" limits="" for="" control="" room="" operators.="" the="" maximum="" allowable="" iodine="" specific="" activity="" is="" not="" associated="" with="" any="" initiating="" event="" and,="" therefore,="" cannot="" affect="" the="" probability="" of="" any="" accident.="" the="" proposed="" amendments="" result="" in="" a="" more="" conservative="" action="" limit="" and,="" therefore,="" do="" not="" increase="" the="" consequences="" of="" any="" accident.="" 2.="" the="" proposed="" amendments="" would="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" proposed="" amendments="" conservatively="" reduce="" the="" maximum="" allowable="" reactor="" coolant="" iodine="" specific="" activity.="" the="" activity="" limit="" is="" not="" associated="" with="" any="" initiating="" event="" and="" the="" system="" design="" is="" not="" affected.="" therefore,="" the="" proposed="" amendments="" cannot="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" 3.="" the="" proposed="" license="" amendments="" do="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" proposed="" amendments="" revise="" action="" statements="" a.1="" and="" a.2="" of="" technical="" specification="" 3/4.4.5="" by="" reducing="" the="" maximum="" allowed="" reactor="" coolant="" specific="" activity="" from="" 4.0="" to="" 3.0="" [microcuries]/gram="" dose="" equivalent="" i-131.="" as="" stated="" above,="" the="" purpose="" of="" the="" maximum="" allowable="" iodine="" specific="" activity="" is="" to="" ensure="" that="" the="" thyroid="" dose="" from="" a="" mslb="" is="" within="" the="" 10="" cfr="" 100="" dose="" guidelines="" and="" the="" general="" design="" criteria="" 19="" dose="" limits="" for="" control="" room="" operators.="" the="" reduction="" in="" the="" activity="" limit="" is="" a="" conservative="" change="" and,="" therefore,="" the="" proposed="" license="" amendments="" do="" not="" involve="" a="" reduction="" in="" the="" margin="" of="" safety.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" university="" of="" north="" carolina="" at="" wilmington,="" william="" madison="" randall="" library,="" 601="" s.="" college="" road,="" wilmington,="" north="" carolina="" 28403-3297.="" attorney="" for="" licensee:="" william="" d.="" johnson,="" vice="" president="" and="" senior="" counsel,="" carolina="" power="" &="" light="" company,="" post="" office="" box="" 1551,="" raleigh,="" north="" carolina="" 27602="" nrc="" project="" director:="" gordon="" e.="" edison,="" acting="" carolina="" power="" &="" light="" company,="" et="" al.,="" docket="" no.="" 50-400,="" shearon="" harris="" nuclear="" power="" plant,="" unit="" 1,="" wake="" and="" chatham="" counties,="" north="" carolina="" date="" of="" amendment="" request:="" june="" 12,="" 1997="" description="" of="" amendment="" request:="" the="" amendment="" would="" make="" changes="" to="" the="" operations="" organization="" description.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" this="" change="" does="" not="" involve="" a="" significant="" hazards="" consideration="" for="" the="" following="" reasons:="" 1.="" the="" proposed="" amendment="" does="" not="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" the="" proposed="" amendment="" deals="" with="" changing="" position="" titles="" and="" clarification="" of="" the="" harris="" nuclear="" plant="" (hnp)="" operations="" management="" organization="" and="" responsibilities.="" the="" changes="" are="" considered="" to="" be="" admnistrative="" in="" nature="" and="" do="" not="" involve="" any="" modifications="" to="" any="" plant="" equipment="" or="" [affect]="" plant="" operation.="" therefore,="" there="" would="" be="" no="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" 2.="" the="" proposed="" amendment="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" proposed="" amendment="" deals="" with="" changing="" position="" titles="" and="" clarification="" of="" the="" hnp="" operations="" management="" organization="" and="" responsibilities.="" the="" changes="" are="" considered="" to="" be="" administrative="" in="" nature="" and="" do="" not="" involve="" any="" modifications="" to="" any="" plant="" equipment="" or="" [affect]="" plant="" operation.="" therefore,="" the="" proposed="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" 3.="" the="" proposed="" amendment="" does="" not="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" the="" proposed="" amendment="" does="" not="" reduce="" the="" margin="" of="" safety="" as="" defined="" in="" the="" safety="" analysis="" report="" or="" the="" bases="" contained="" in="" the="" technical="" specifications.="" the="" requirement="" to="" have="" a="" licensed="" sro="" [senior="" reactor="" operator]="" management="" position="" responsible="" for="" plant="" operations="" is="" maintained="" within="" the="" proposed="" amendment.="" therefore,="" the="" proposed="" change="" does="" not="" involve="" a="" significant="" reduction="" in="" the="" margin="" of="" safety.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" cameron="" village="" regional="" library,="" 1930="" clark="" avenue,="" raleigh,="" north="" carolina="" 27605="" attorney="" for="" licensee:="" william="" d.="" johnson,="" vice="" president="" and="" senior="" counsel,="" carolina="" power="" &="" light="" company,="" post="" office="" box="" 1551,="" raleigh,="" north="" carolina="" 27602="" nrc="" project="" director:="" gordon="" e.="" edison,="" acting="" [[page="" 40848]]="" commonwealth="" edison="" company,="" docket="" nos.="" 50-373="" and="" 50-374,="" lasalle="" county="" station,="" units="" 1="" and="" 2,="" lasalle="" county,="" illinois="" date="" of="" amendment="" request:="" may="" 27,="" 1997="" description="" of="" amendment="" request:="" the="" proposed="" amendments="" would="" revise="" technical="" specification="" section="" 6,="" ``administrative="" controls,''="" to="" incorporate="" revised="" organizational="" titles="" and="" would="" modify="" license="" condition="" 2.c.(30)(a)="" to="" reflect="" that="" the="" shift="" technical="" advisor="" function="" may="" be="" filled="" by="" someone="" other="" than="" a="" designated="" senior="" reactor="" operator="" (sro).="" in="" addition,="" the="" proposed="" amendments="" would="" change="" the="" submittal="" frequency="" of="" the="" radiological="" effluent="" release="" report="" from="" semiannually="" to="" annually.="" the="" proposed="" amendments="" will="" also="" make="" several="" administrative="" and="" editorial="" changes.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" a.="" the="" proposed="" changes="" do="" not="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" the="" proposed="" changes="" do="" not="" affect="" any="" accident="" initiators="" or="" precursors="" and="" do="" not="" change="" or="" alter="" the="" design="" assumptions="" for="" systems="" or="" components="" used="" to="" mitigate="" the="" consequences="" of="" an="" accident.="" the="" proposed="" changes="" do="" not="" affect="" the="" design="" or="" operation="" of="" any="" system,="" structure,="" or="" component="" in="" the="" plant.="" there="" are="" no="" changes="" to="" parameters="" governing="" plant="" operation,="" and,="" no="" new="" or="" different="" type="" of="" equipment="" will="" be="" installed.="" the="" proposed="" changes="" provide="" clarification,="" consistency="" with="" station="" procedures,="" programs,="" the="" code="" of="" federal="" regulations="" (10cfr),="" other="" technical="" specifications,="" and="" improved="" technical="" specifications.="" these="" changes="" do="" not="" impact="" any="" accident="" previously="" evaluated="" in="" the="" ufsar="" [updated="" final="" safety="" analysis="" report].="" there="" is="" no="" relaxation="" of="" applicable="" administrative="" controls.="" those="" administrative="" requirements="" which="" have="" no="" effect="" on="" safe="" operation="" of="" the="" plant="" are="" eliminated.="" b.="" the="" proposed="" changes="" do="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" proposed="" changes="" do="" not="" affect="" the="" design="" or="" operation="" of="" any="" plant="" system,="" structure,="" or="" component.="" there="" are="" no="" changes="" to="" parameters="" governing="" plant="" operation,="" and,="" no="" new="" or="" different="" type="" of="" equipment="" will="" be="" installed.="" the="" organizational="" and="" administrative="" changes="" proposed="" have="" no="" effect="" on="" the="" design="" or="" operation="" of="" any="" system,="" structure,="" or="" component="" in="" the="" plant.="" there="" are="" no="" changes="" to="" parameters="" governing="" plant="" operation;="" no="" new="" or="" different="" type="" of="" equipment="" will="" be="" installed.="" c.="" the="" proposed="" changes="" do="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" proposed="" changes="" do="" not="" affect="" the="" margin="" of="" safety="" for="" any="" technical="" specification.="" the="" initial="" conditions="" and="" methodologies="" used="" in="" the="" accident="" analyses="" remain="" unchanged;="" therefore,="" accident="" analyses="" results="" are="" not="" impacted.="" plant="" safety="" parameters="" or="" setpoints="" are="" not="" affected.="" all="" responsibilities="" described="" in="" the="" technical="" specifications="" for="" administrative="" controls="" will="" continue="" to="" be="" performed="" by="" individuals="" possessing="" the="" requisite="" qualifications.="" clarifications,="" relocations,="" and="" nomenclature="" changes="" neither="" result="" in="" a="" reduction="" of="" personnel="" responsibilities,="" nor="" do="" they="" cause="" a="" relaxation="" of="" programmatic="" controls.="" there="" are="" no="" resulting="" effects="" on="" plant="" safety="" parameters="" or="" setpoints.="" guidance="" has="" been="" provided="" in="" ``final="" procedures="" and="" standards="" on="" no="" significant="" hazards="" considerations,''="" final="" rule,="" 51="" fr="" 7744,="" for="" the="" application="" of="" standards="" to="" license="" change="" requests="" for="" determination="" of="" the="" existence="" of="" significant="" hazards="" considerations.="" this="" document="" provides="" examples="" of="" amendments="" which="" are="" and="" are="" not="" considered="" likely="" to="" involve="" significant="" hazards="" considerations.="" these="" proposed="" amendments="" most="" closely="" fit="" the="" example="" of="" a="" purely="" administrative="" change="" to="" the="" technical="" specifications="" to="" achieve="" consistency="" throughout="" the="" technical="" specifications,="" correction="" of="" an="" error,="" or="" a="" change="" in="" nomenclature.="" the="" proposed="" amendment="" does="" not="" involve="" a="" significant="" relaxation="" of="" the="" criteria="" used="" to="" establish="" safety="" limits,="" a="" significant="" relaxation="" of="" the="" bases="" for="" the="" limiting="" safety="" system="" settings,="" or="" a="" significant="" relaxation="" of="" the="" bases="" for="" the="" limiting="" conditions="" for="" operations.="" the="" proposed="" change="" does="" not="" reduce="" the="" margin="" of="" safety="" as="" defined="" in="" the="" basis="" for="" any="" technical="" specification.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" requested="" amendments="" involve="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" jacobs="" memorial="" library,="" illinois="" valley="" community="" college,="" oglesby,="" illinois="" 61348="" attorney="" for="" licensee:="" michael="" i.="" miller,="" esquire;="" sidley="" and="" austin,="" one="" first="" national="" plaza,="" chicago,="" illinois="" 60603="" nrc="" project="" director:="" robert="" a.="" capra="" commonwealth="" edison="" company,="" docket="" nos.="" 50-373="" and="" 50-374,="" lasalle="" county="" station,="" units="" 1="" and="" 2,="" lasalle="" county,="" illinois="" date="" of="" amendment="" request:="" july="" 1,="" 1997="" description="" of="" amendment="" request:="" the="" proposed="" amendments="" would="" change="" the="" definition="" of="" channel="" calibration="" in="" section="" 1.4="" of="" the="" technical="" specifications="" to="" require="" an="" inplace="" qualitative="" assessment="" of="" thermocouple="" and="" resistance="" temperature="" detectors="" which="" cannot="" be="" calibrated.="" the="" proposed="" amendments="" will="" also="" correct="" typographical="" and="" miscellaneous="" errors="" in="" ts="" table="" 3.3.2-1,="" table="" 3.3.6-1,="" and="" bases="" section="" 3/4.3.1.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" 1)="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" because:="" a.="" the="" change="" in="" the="" definition="" of="" a="" channel="" calibration="" is="" to="" make="" the="" wording="" more="" clear="" and="" to="" require="" an="" inplace="" qualitative="" assessment="" in="" place="" of="" the="" calibration="" of="" thermocouple="" and="" resistance="" temperature="" detector="" (rtd)="" sensors.="" the="" thermocouple="" and="" rtd="" sensors="" are="" not="" adjustable="" and="" are="" not="" subject="" to="" drift="" due="" to="" their="" design.="" the="" inplace="" qualitative="" assessments="" will="" assure="" proper="" functioning="" of="" the="" sensors,="" due="" to="" the="" nature="" of="" these="" sensors="" and="" the="" associated="" failure="" modes,="" and="" thus="" will="" verify="" that="" the="" sensors="" will="" be="" able="" to="" fulfill="" their="" intended="" function(s).="" therefore="" the="" change="" to="" the="" definition="" will="" not="" change="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" b.="" manual="" initiation="" of="" isolation="" actuation="" instrumentation="" trip="" systems="" for="" inboard="" and="" outboard="" valves="" is="" required="" to="" be="" operable="" per="" ts="" table="" 3.3.2-1,="" trip="" functions="" b.1="" and="" b.2,="" respectively.="" trip="" function="" b.2,="" outboard="" valves,="" lists="" valve="" group="" 7,="" tip="" system="" isolation="" valves.="" valve="" group="" 7="" consists="" of="" an="" automatic="" inboard="" isolation="" valve="" for="" each="" tip="" guide="" tube="" penetrating="" the="" primary="" containment="" (correctly="" listed="" under="" b.1),="" and="" a="" manual="" outboard="" isolation="" valve="" on="" each="" guide="" tube,="" that="" is="" an="" explosive="" squib="" valve.="" each="" explosive="" squib="" valve="" is="" manually="" actuated="" with="" a="" keylock="" switch="" from="" the="" main="" control="" room="" per="" design.="" each="" is="" a="" positive="" control="" backup="" upon="" failure="" of="" an="" inboard="" valve="" in="" the="" open="" position.="" the="" squib="" valves="" are="" not="" actuated="" from="" isolation="" actuation="" channel="" logic.="" this="" configuration="" meets="" the="" current="" design="" and="" licensing="" basis.="" therefore,="" deletion="" of="" valve="" group="" 7="" from="" ts="" table="" 3.3.2-1="" will="" not="" change="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" c.="" the="" proposed="" change="" to="" ts="" table="" 3.3.6-1,="" control="" rod="" withdrawal="" block="" instrumentation,="" deletes="" note="" (e)="" from="" trip="" function="" 4.a,="" irm="" detector-not-full-in="" rod="" block.="" this="" rod="" withdrawal="" block="" functions="" during="" operational="" condition="" 2,="" startup,="" and="" 5,="" refuel,="" to="" assure="" that="" irms="" are="" operable="" during="" control="" rod="" withdrawal="" in="" these="" plant="" operational="" conditions.="" the="" rod="" block="" is="" not="" bypassed="" when="" the="" irms="" are="" on="" range="" 1.="" thus="" note="" (e)="" does="" not="" apply="" to="" this="" trip="" function="" and="" is="" being="" deleted.="" therefore,="" the="" correction="" of="" this="" error="" will="" not="" change="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" [[page="" 40849]]="" d.="" the="" change="" to="" ts="" bases="" 3/4.3.1="" to="" correct="" a="" typographical="" error="" referencing="" ts="" table="" 3.3.1-2,="" note="">, instead of Note 
     is an administrative change and thus will not 
    change the probability or consequences of an accident.
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        The changes to the definition of Channel Calibration and 
    correction of the other miscellaneous errors in the TS and TS Bases 
    will not create the possibility of a new or different kind of 
    accident, because the changes will not affect the design or 
    operation of any structure, system, or component in the plant.
        3) Involve a significant reduction in the margin of safety 
    because:
        a. The definition of Channel Calibration is being changed to be 
    like the definition in NUREG 1434, Standard Technical Specifications 
    General Electric Plants, BWR/6, Revision 1. The primary changes 
    involve requiring only an inplace qualitative assessment of 
    thermocouple and RTD sensors. These sensors are not adjustable and 
    not susceptible to setpoint drift. Thus the appropriate check of the 
    sensors is a qualitative assessment only. The inplace qualitative 
    assessment assures operability of the sensors. Therefore there is no 
    reduction in the margin of safety.
        b. The remaining miscellaneous changes are corrections due to 
    errors in the TS. The corrections will make the associated TS 
    consistent with the design and licensing basis of LaSalle or correct 
    typographical errors. Therefore, there is no reduction in the margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: July 17, 1996, as supplemented by 
    letters dated June 3, and July 7, 1997.
        Description of amendment request: The proposed change request 
    modifies Waterford Steam Electric Station, Unit 3, Technical 
    Specifications (TSs) 3/4.7.1.3, ``CONDENSATE STORAGE POOL,'' by 
    increasing the minimum Condensate Storage Pool (CSP) level from 82 
    percent to 91 percent in Modes 1, 2, and 3. The July 7, 1997, 
    supplement proposes to expand the applicability of TS 3.7.1.3 to 
    include Mode 4 operational requirements and maintains the 91 percent 
    minimum CSP level previously requested for Modes 1, 2, and 3. The staff 
    previously issued No Significant Hazard Considerations notice on March 
    26, 1997 (62 FR 14461).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?Response: No.
        Increasing the minimum required Condensate Storage Pool (CSP) 
    level to 91 percent will insure that the minimum required 170,000 
    gallons of water is available to supply the Emergency Feedwater 
    System and that 3,500 gallons of water is available for use by the 
    Component Cooling Water Makeup System in Modes 1, 2, and 3. 
    Maintaining a minimum required CSP level of 11 percent will insure 
    that 3,500 gallons of water is available for use by the Component 
    Cooling Water Makeup System in Mode 4. Maintaining the minimum 
    required water volume will not increase the probability of any 
    accident previously evaluated. Additionally, it will not affect the 
    consequences of any accident. Maintaining a minimum required CSP 
    level will ensure that the system remains within the bounds of the 
    accident analysis. Therefore, the proposed change will not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        Increasing the minimum water volume of the CSP from 82 percent 
    to 91 percent in Modes 1, 2, and 3 does not create a possibility for 
    a new or different kind of accident. Maintaining a minimum water 
    volume of the CSP at 11 percent in Mode 4 does not create a 
    possibility for a new or different kind of accident. The CSP will be 
    operated in the same manner as previously evaluated. Therefore, the 
    proposed change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        Operation in accordance with this proposed change will ensure 
    that the minimum contained water volume of the CSP will remain 
    adequate under all conditions. This will improve the present margin 
    of safety. Therefore, the proposed change will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: James W. Clifford, Acting Director
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: May 29, 1997
        Description of amendment request: The proposed amendments will 
    improve consistency throughout the Technical Specifications and their 
    related Bases by removing outdated material, incorporating minor 
    changes in text, making editorial corrections, and resolving other 
    inconsistencies identified by the licensee's plant operations staff.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments consist of administrative changes to the 
    Technical Specifications (TS) for St. Lucie Units 1 and 2. The 
    amendments will implement minor changes in text to rectify 
    reference, typographic, spelling, and/or consistency-in-format 
    errors; update the TS Bases; and/or otherwise improve consistency 
    within the TS for each unit. The proposed amendments do not involve 
    changes to the configuration or method of operation of 
    plantequipment that is used to mitigate the consequences of an 
    accident, nor do the changes otherwise affect the initial conditions 
    or conservatisms assumed in any of the plant accident analyses. 
    Therefore, operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
    
    [[Page 40850]]
    
        The proposed administrative revisions will not change the 
    physical plant or the modes of plant operation defined in the 
    Facility License for each unit. The changes do not involve the 
    addition or modification of equipment nor do they alter the design 
    or operation of plant systems. Therefore, operation of the facility 
    in accordance with the proposed amendments would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed amendments are administrative in nature and do not 
    change the basis for any technical specification that is related to 
    the establishment of, or the preservation of, a nuclear safety 
    margin. Therefore, operation of the facility in accordance with the 
    proposed amendments would not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420
        NRC Project Director: Frederick J. Hebdon
    
    GPU Nuclear Corporation, Docket No. 50-320, Three Mile Island 
    Nuclear Station, Unit No. 2 (TMI-2), Dauphin County, Pennsylvania
    
        Date of amendment request: December 2, 1996
        Description of amendment request: The proposed amendment would 
    relocate the audit frequency requirements from the plant Technical 
    Specifications to the Quality Assurance Plan. In addition, the maximum 
    interval between certain types of audits will be extended. This change 
    would make the TMI-2 technical specifications consistent with the 
    Technical Specifications for Three Mile Island, Unit 1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        10 CFR 50.92 provides the criteria which the Commission uses to 
    perform a No Significant Hazards Consideration. 10 CFR 50.92 states 
    that an amendment to a facility license involves No Significant 
    Hazards if operation of the facility in accordance with the proposed 
    amendment would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, or
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. Involve a significant reduction in a margin of safety.
        The proposed change to the technical specifications is 
    administrative and does not involve any physical changes to the 
    facility. No changes are made to operating limits or parameters, nor 
    to any surveillance activities. Based on this, GPU Nuclear has 
    concluded that the proposed change does not:
        1. Involve a significant increase in the probability of 
    occurrence of the consequences of an accident previously evaluated.
        The proposed amendment is administrative and does not affect the 
    function of any system or component. Therefore this change does not 
    increase the probability of occurrence or the consequences of an 
    accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed change is administrative and no new failure modes 
    or potential accident scenarios are created.
        3. Involve a change in the margin of safety.
        This change is administrative in nature and does not affect any 
    safety settings, equipment, or operational parameters.
        Based on the above analysis it is concluded that the proposed 
    changes involve no significant safety hazards considerations as 
    defined by 10 CFR 50.92.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW, Washington, D.C. 20037 
    NRC Project Acting Director: Marvin M. Mendonca
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: July 16, 1997
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Table 2.2-1 and 3/4.2.5 to allow the 
    reactor coolant system total flow to be determined using cold leg elbow 
    tap differential pressure measurements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Pursuant to 10[]CFR[]50.92 each application for amendment to an 
    operating license must be reviewed to determine if the proposed 
    change involves a Significant Hazards Consideration. The amendment, 
    as defined below, describing the Technical Specification change 
    associated with the change has been reviewed and determined to not 
    involve Significant Hazards Considerations. The basis for this 
    determination follows.
        Proposed Change: The current Technical Specification Table 2.2-1 
    (page 2-4) ``Reactor Trip System Instrumentation Trip Setpoints,'' 
    provides the Trip Setpoint and Allowable Value for the RCS [reactor 
    coolant system] Flow-Low trip. The Allowable Value will be changed 
    to reflect the increased uncertainty associated with the correlation 
    of the elbow taps to a previous baseline calorimetric. In addition, 
    Technical Specification 3.2.5 (page 3/4.2-11), ``Power Distribution 
    Limits, DNB Parameters'', will be changed to allow the RCS total 
    flow to be measured by the elbow tap [delta]p method. These changes 
    will include the modification of surveillance requirement 4.2.5.3, 
    which currently requires performance of a precision heat balance 
    every 18 months, to allow use of the elbow tap [delta]p method for 
    RCS flow measurement. Appropriate Technical Specification Bases 
    sections will also be revised to reflect use of the elbow tap 
    [delta]p method for flow measurement and to provide clarification. 
    The revised Technical Specifications are in Appendix C.
        Background: The 18-month total RCS flow surveillance is 
    typically satisfied by a secondary power calorimetric-based RCS flow 
    measurement. In recent cycles, South Texas Project has experienced 
    apparent decreases in flow rates which have been attributed to 
    variations in hot leg streaming effects. These effects directly 
    impact the hot leg temperatures used in the precision calorimetric, 
    resulting in the calculation of low RCS flow rates. The apparent 
    flow reduction has become more pronounced in fuel cycles which have 
    implemented aggressive low leakage loading patterns. Evidence that 
    the flow reduction was apparent, but not actual, was provided by 
    elbow tap measurements. The results of this evaluation, including a 
    detailed description of the hot leg streaming phenomenon, are 
    documented in Westinghouse report SAE/FSE-TGX/THX-0152, ``RCS Flow 
    Verification Using Elbow Taps.''
        South Texas Project intends to begin using an alternate method 
    of measuring RCS flow using the elbow tap [delta]p measurements. For 
    this alternate method, the RCS elbow tap measurements are correlated 
    to precision
    
    [[Page 40851]]
    
    calorimetric measurements performed during earlier cycles which 
    decreased the effects of hot leg streaming.
        The purpose of this evaluation is to assess the impact of using 
    the elbow tap [delta]p measurements as an alternate method for 
    performing the 18-month RCS flow surveillance on the licensing basis 
    and demonstrate that it will not adversely affect the subsequent 
    safe operation of the plant. This evaluation supports the conclusion 
    that implementation of the elbow tap [delta]p measurement as an 
    alternate method of determining RCS total flow rate does not 
    represent a significant hazards consideration as defined in 
    10[]CFR[]50.92.
        Evaluation: Use of the elbow tap [delta]p method to determine 
    RCS total flow requires that the [delta]p measurements for the 
    present cycle be correlated to the precision calorimetric flow 
    measurement which was performed during the baseline cycle(s). A 
    calculation has been performed to determine the uncertainty in the 
    RCS total flow using this method. This calculation includes the 
    uncertainty associated with the RCS flow baseline calorimetric 
    measurement, as well as uncertainties associated with [delta]p 
    transmitters and indication via QDPS [qualified display processing 
    system] or the plant process computer. The uncertainty calculation 
    performed for this method of flow measurement is consistent with the 
    methodology recommended by the Nuclear Regulatory Commission (NUREG/
    CR-3659, PNL-4973, 2/85). The only significant difference is the 
    assumption of correlation to a previously performed RCS flow 
    calorimetric. However, this has been accounted for by the addition 
    of instrument uncertainties previously considered to be zeroed out 
    by the assumption of normalization to a calorimetric performed each 
    cycle. Based on these calculations, the uncertainty on the RCS flow 
    measurement using the elbow tap method is 2.6% flow which results in 
    a minimum RCS total flow of 391,500 gpm and must be measured via 
    indication with QDPS or the plant process computer at approximately 
    100% power.
        The specific calculations performed were for Precision RCS Flow 
    Calorimetrics for the specified baseline cycles, Indicated RCS Flow 
    (either QDPS or the plant process computer), and the Reactor Coolant 
    Flow - Low reactor trip. The calculations for Indicated RCS Flow and 
    Reactor Coolant Flow - Low reactor trip reflect correlation of the 
    elbow taps to baseline precision RCS Flow Calorimetrics. As 
    discussed above, additional instrument uncertainties were included 
    for this correlation.
        The uncertainty associated with the RCS Flow - Low trip 
    increased slightly. It was determined that due to the availability 
    of margin in the uncertainty calculation, no change was necessary to 
    either the Trip Setpoint (91.8% flow) or to the current Safety 
    Analysis Limit (87% flow) to accommodate this increase. The 
    Allowable Value is to be modified to allow for the increased 
    instrument uncertainties associated with the [delta]p to flow 
    correlation.
        Since the flow uncertainty did not increase over the currently 
    analyzed value, no additional evaluations of the reactor core safety 
    limits must be performed. In addition, it was determined that the 
    current Minimum Measured Flow (MMF) assumed in the safety analyses 
    (389,200 gpm) bounds the required MMF calculated for the elbow tap 
    method (391,500 gpm).
        Based on these evaluations, the proposed change would not 
    invalidate the conclusions presented in the UFSAR [Updated Final 
    Safety Analysis Report].
        1. Does the proposed modification involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated?
        Sufficient margin exists to account for all reasonable 
    instrument uncertainties; therefore, no changes to installed 
    equipment or hardware in the plant are required, thus the 
    probability of an accident occurring remains unchanged.
        The initial conditions for all accident scenarios modeled are 
    the same and the conditions at the time of trip, as modeled in the 
    various safety analyses, are the same. Therefore, the consequences 
    of an accident will be the same as those previously analyzed.
        2. Does the proposed modification create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated?
        The proposed change revises the method for RCS flow measurement, 
    and therefore does not introduce any new accident indicators or 
    failure mechanisms.
        No new accident scenarios have been identified. Operation of the 
    plant will be consistent with that previously modeled, i.e., the 
    time of reactor trip in the various safety analyses is the same, 
    thus plant response will be the same and will not introduce any 
    different accident scenarios that have not been evaluated.
        3. Does the proposed modification involve a significant 
    reduction in a margin of safety[?]
        There are no changes to the Safety Analysis assumptions. 
    Therefore, the margin of safety will remain the same.
        The proposed change does not impact the results from any 
    accidents analyzed in the safety analysis.
        Conclusion: Based on the preceding information, it has been 
    determined that this proposed change to allow an alternate RCS total 
    flow measurement based on elbow tap [delta]p measurements does not 
    involve a Significant Hazards Consideration as defined by 10 CFR 
    50.92(c).
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869
        NRC Project Director: James W. Clifford, Acting
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station, Unit 1, Oswego County, New York
    
        Date of amendment request: July 2, 1997
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) 3/4.2.3 regarding reactor coolant 
    chemistry in accordance with a report by Electrical Power Research 
    Institute, Inc. (EPRI) TR-103515-R1, ``BWR Water Chemistry Guidelines, 
    1996 Revision,'' also known as Boiling Water Reactor Vessel and 
    Internals Project (BWRVIP)-29. Specifically, the amendment would define 
    new conductivity limits in TS 3.2.3a (when reactor coolant is 200 
    degrees F or more and reactor thermal power is no more that 10%), and 
    in TS 3.2.3b (when reactor thermal power exceeds 10%). The new 
    conductivity limits would be 1 micro-mho/cm, which is less than the 
    existing limits of 2 micro-mho/cm and 5 micro-mho/cm. The chloride ion 
    limit in TS 3.2.3a, 0.1 ppm, would remain at this value but would be 
    designated as 100 ppb. The chloride ion limit in TS 3.2.3b would be 
    changed from 0.2 ppm to 20 ppb. Sulfate ion limits would be added to TS 
    3.2.3a and TS 3.2.3b at 100 ppb and 20 ppb, respectively. In TS 3.2.3c, 
    the maximum conductivity limit would be changed from 10 micro-mho/cm to 
    5 micro mho/cm when reactor coolant temperature is 200 degrees F or 
    more; the maximum chloride ion concentration limit would be changed 
    from 0.5 ppm to 100 ppb (when reactor thermal power exceeds 10%) and 
    200 ppb (when reactor coolant temperature is 200 degrees F or more and 
    reactor thermal power is no more than 10%); and the maximum sulfate ion 
    concentration of 100 ppb (when reactor thermal power exceeds 10%) and 
    200 ppb (when reactor coolant temperature is 200 degrees F or more and 
    reactor thermal power is no more than 10%) would be added. The 
    requirement to place the reactor in the cold shutdown condition as 
    currently specified in TS 3.2.3d (when TSs 3.2.2a, b, and c are not 
    met) and TS 3.2.3e (when the continuous conductivity monitor is 
    inoperable for more than 7 days) would be changed to require that the 
    reactor coolant temperature be reduced to below 200 degrees F. TS 4.2.3 
    would be revised to add that the samples taken and analyzed for 
    conductivity and chloride ion content are also to be analyzed for 
    sulfate ion content. TS Bases 3/4.2.3 would also be changed to
    
    [[Page 40852]]
    
    reflect that the purpose of TS 3/4.2.3 is to limit crack growth rates 
    to values consistent with Unit 1 core shroud analyses in accordance 
    with an NRC letter dated May 8, 1997.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Nine Mile Point Unit 1, in accordance with 
    the proposed amendment, will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The changes to the conductivity and chloride ion action levels 
    and the addition of sulfate ion levels as an action level in reactor 
    water chemistry are being made to make the TS and its Bases 
    consistent with the values used in the core shroud vertical weld 
    cracking evaluations. These new values reflect the BWR water 
    chemistry guidelines, 1996 revision (EPRI TR-103515-R1, BWRVIP-29) 
    and are equal to or more restrictive than the present TS values. No 
    physical modification of the plant is involved and no changes to the 
    methods in which plant systems are operated are required. None of 
    the precursors of previously evaluated accidents are affected and 
    therefore, the probability of an accident previously evaluated is 
    not increased. These changes to the coolant chemistry TS are more 
    restrictive limits and no new failure modes are introduced. 
    Therefore, these changes will not involve a significant increase in 
    the consequences of an accident previously evaluated.
        2. The operation of Nine Mile Point Unit 1, in accordance with 
    the proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The changes to the conductivity and chloride ion action levels 
    and the addition of sulfate ion levels as an action level in reactor 
    water chemistry are being made to make the TS and its Bases 
    consistent with the values use in the core shroud vertical weld 
    cracking evaluations. The new values reflect the BWR water chemistry 
    guidelines, 1996 revision (EPRI TR-103515-R1, BWRVIP-29) and are 
    equal to or more restrictive than the present TS values. No physical 
    modification of the plant is involved and no changes to the methods 
    in which plant systems are operated are required. The change does 
    not introduce any new failure modes or conditions that may create a 
    new or different accident. Therefore, this change does not create 
    the possibility of a new or different kind of accident [from any 
    accident] previously evaluated.
        3. The operation of Nine Mile Point Unit 1, in accordance with 
    the proposed amendment, will not involve a significant reduction in 
    a margin of safety.
        The changes to the conductivity and chloride ion action levels 
    and the addition of sulfate ion levels as an action level in reactor 
    water chemistry are being made to make the TS and its Bases 
    consistent with the values used in the core shroud vertical weld 
    cracking evaluations. These new values reflect the BWR water 
    chemistry guidelines, 1996 revision (EPRI TR-103515-R1, BWRVIP-29) 
    and are equal to or more restrictive than the present TS values. No 
    physical modification of the plant is involved and no changes to the 
    methods in which plant systems are operated are required. This 
    change does not adversely affect any physical barrier to the release 
    of radiation to plant personnel or the public. Therefore, the change 
    does not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: Alex Dromerick, Acting
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: June 19, 1997
        Description of amendment request: Technical Specification Table 
    2.2-1 Notes 1 and 3 define the values for the constants used in the 
    Overtemperature Delta-T and Overpower Delta-T reactor trip system 
    instrumentation setpoint calculators. The proposed amendment would make 
    changes to the notes as well as the associated Bases section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 
    10CFR50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed revision does not involve an SHC because the 
    revision would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes to Technical Specification Table 2.2-1 
    Notes 1 and 3 for the addition of the inequalities ensure that the 
    constants used for [Overtemperature Delta-T] and [Overpower Delta-T] 
    will be set conservatively with respect to the assumptions in the 
    accident analysis. The effect on the turbine
        runback function has been evaluated with respect to the Loss of 
    External Electrical Load And/Or Turbine Trip analysis and it has 
    been determined that this change does not increase the probability 
    of this transient. The change was also reviewed to determine if it 
    produced an increase in the probability of an unnecessary or 
    spurious reactor trip and it was determined that it did not. This 
    change does not increase the probability of any previously evaluated 
    accident.
        The consequences of previously evaluated accidents, including 
    Uncontrolled Rod Cluster Assembly Bank Withdrawal At Power, Rod 
    Cluster Control Assembly Misalignment, Uncontrolled Boron Dilution, 
    Loss of External Electrical Load And/Or Turbine Trip, Excessive Heat 
    Removal Due To Feedwater System Malfunctions, Excessive Load 
    Increase Incident, Accidental Depressurization Of The Reactor 
    Coolant System, Accidental Depressurization Of The Main Steam 
    System, Loss of Reactor Coolant From Small Ruptured Pipes Or From 
    Cracks In Large Pipes Which Actuate ECCS [emergency core cooling 
    system], or Major Secondary System Pipe Ruptures have not changed.
        The administrative changes have no impact on the design or 
    operation of Millstone Unit 3.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to Technical Specification Table 2.2-1 
    Notes 1 and 3 do not alter the design, construction, operation, 
    maintenance or method of testing of equipment. The proposed changes 
    alter the Technical Specification description of [an] 
    [Overtemperature Delta-T] and [Overpower Delta-T] setpoint functions 
    and requires only slight changes to the actual setpoints in the 
    field. The [Overtemperature Delta-T] and [Overpower Delta-T] 
    functions serve to mitigate the effects of accidents by opening the 
    Reactor Trip breakers or reduce power by ``running back'' turbine 
    electrical load. The change does not create any new interfaces to 
    plant control or protection systems and therefore, no new mechanism 
    for accident initiation has been introduced. The proposed change 
    does not introduce the possibility of an accident of a different 
    type than previously evaluated.
        Therefore, the proposed revision does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to Technical Specification Table 2.2-1 
    Notes 1 and 3 do not affect the integrity of any physical fission 
    protective boundaries, increase the delays in actuation of safety 
    systems beyond that assumed in the safety analysis or reduce the
    
    [[Page 40853]]
    
    margin of safety of any system. These changes ensure that actuation 
    of Overtemperature [Delta-T] and Overpower [Delta-T] reactor trips 
    will occur conservatively with respect to the assumptions of the 
    accident analysis.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Deputy Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: June 19, 1997
        Description of amendment request: Technical Specification 3/4.7.1.3 
    requires sufficient water to be available for the auxiliary feedwater 
    (AFW) system to maintain the reactor coolant system at hot standby for 
    10 hours before cooling down to hot shutdown in the next 6 hours. The 
    proposed amendment would increase the required volume of water when the 
    condensate storage tank is used, make editorial changes, and expand the 
    description in the appropriate Bases section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 
    10CFR50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed revision does not involve an SHC because the 
    revision would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed change to Technical Specification Surveillance 
    4.7.1.3.2 will account for the unusable Condensate Storage Tank 
    (CST) inventory by increasing the required combined CST and 
    Demineralized Water Storage Tank (DWST) inventory to 384,000 
    gallons. The increased required water volume is consistent with the 
    design of the CST and will provide assurance that sufficient water 
    is available to maintain the reactor coolant system at Hot Standby 
    for 10 hours before cooling down to Hot Shutdown in the next 6 
    hours.
        The proposed changes to reword Technical Specification 3/
    4.7.1.3, expand the description in Bases Section B3/4.7.1.3 and 
    modify the description in Bases Section B3/4.7.1.2 are to update and 
    clarify the requirements.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to Technical Specification 3/4.7.1.3 do not 
    change the use of DWST or CST during normal or accident evaluations.
        The proposed changes to reword Technical Specification 3/
    4.7.1.3, Bases Section B3/4.7.1.3 and Bases Section B3/4.7.1.2 are 
    to update and clarify the requirements.
        Therefore, the proposed revision does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to Technical Specification Surveillance 
    4.7.1.3.2 will increase the required inventory for the combined CST 
    and DWST to account for an additional 50,000 gallons of unusable 
    inventory due to the CST discharge line location, other physical 
    characteristics, and measurement uncertainty. The proposed change to 
    the surveillance requirement will increase the required volume of 
    the combined CST and DWST inventory to 384,000 gallons. The proposed 
    change ensures that sufficient water is available to maintain the 
    Reactor Coolant System at Hot Standby conditions for 10 hours with 
    steam discharge to the atmosphere, concurrent with a total loss-of-
    offsite power, and with an additional 6-hour cool down period to 
    reduce reactor coolant temperature to 350 [degrees] F.
        The proposed changes to Technical Specification 3/4.7.1.3 and 
    Bases Section 3/4.7.1.3 are to clarify the requirements. The 
    proposed changes to the Bases Section 3/4.7.1.2 update and expands 
    the description of the design bases accidents for which AFW System 
    is credited for accident mitigation. This additional information is 
    consistent with the current AFW System design bases.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location:  Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Deputy Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: June 30, 1997
        Description of amendment request: Technical Specification 
    Surveillance Requirements 4.7.1.5.1 and 4.7.1.5.2 require the periodic 
    testing of the main steam isolation valves (MSIVs) to demonstrate 
    operability. The proposed amendment would (1) clarify when the MSIVs 
    are partial stroked or full closure tested, (2) add a note to the Mode 
    4 applicability of Technical Specification 3.7.1.5 to require that the 
    MSIVs be closed and deactivated at less than 320 degrees F, (3) make 
    editorial changes, and (4) make changes to the associated Bases 
    sections.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 
    10CFR50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed revision does not involve [an] SHC because 
    the revision would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed changes to Technical Specifications Surveillances 
    4.7.1.5.1 and 4.7.1.5.2 are to clarify the testing of the MSIVs by 
    rewording and separating the requirements into three surveillances.
    
    [[Page 40854]]
    
    Currently, Technical Specifications Surveillance 4.7.1.5.1 requires 
    ``verifying full closure within 10 seconds ... in MODES 1, 2, and 3 
    when tested pursuant to Specification 4.0.5.'' The current 
    surveillance requirement to full stroke test the MSIVs is not 
    performed during power operation as the Millstone Unit 3 Inservice 
    Pump and Valve Test Program pursuant to Specification 4.0.5, has 
    received relief from the quarterly full stroke surveillance testing 
    requirement. The basis for the relief is that full stroking the 
    MSIVs to the closed position during power operation would result in 
    an unbalanced steam flow condition producing an abnormal power 
    distribution in the reactor core, possibly causing a reactor trip. 
    The MSIVs are equipped with provisions for inservice testing by 
    partial stroking. The partial stroking is accomplished by opening a 
    solenoid valve to admit steam pressure into the lower piston 
    chamber. After a time delay the solenoid valve for the upper piston 
    chamber opens. After 10 percent travel the position indicating 
    device vents both piston chambers and the valve fully opens to the 
    back seat due to pressure acting on the valve plug. The accepted 
    alternate testing method is to partially stroke test the MSIVs 
    during power operation and full stroke test the valves during 
    shutdowns.
        The proposed changes to Technical Specifications Surveillance 
    4.7.1.5.2 will identify a Mode 3 requirement to perform a 10 second 
    full closure test of the MSIVs in Mode 3 or 4. Surveillance 
    4.7.1.5.3 will identify a Mode 4 requirement to perform a 120 second 
    full closure test of the MSIVs in Mode 4 when the RCS [reactor 
    coolant system] temperature is greater than or equal to 320 degrees 
    F. The 320 degrees F restriction on testing the valves is consistent 
    with recommendations from the valve manufacturer. Additionally, a 
    footnote is added to the LCO [limiting condition for operation] and 
    the surveillance to identify that the MSIVs are required to be 
    closed and deactivated when the RCS temperature is less than 320 
    degrees F.
        The proposed changes are consistent with equipment design and 
    the surveillance testing of the MSIVs provides the necessary 
    assurance that the valves will function consistent with accident 
    analyses.
        The other proposed changes to reword the Applicability and 
    Action statements of Technical Specification 3.7.1.5 and Bases 
    Section B3/4.7.1.5 are considered administrative changes.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to the surveillance testing of the MSIVs 
    does not change the operation of the valves as assumed for accident 
    analyses. The MSIVs are currently equipped with provisions for 
    partial stroking.
        Therefore, the proposed revision does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to Technical Specifications Surveillances 
    4.7.1.5.1 and 4.7.1.5.2 are to clarify the testing of the MSIVs by 
    rewording and separating the requirements into three surveillances. 
    Surveillance 4.7.1.5.1 will identify a Mode 1 and 2 requirement to 
    partial stroke test the MSIVs in Mode 1 and 2 unless a successful 10 
    second full stroke test was performed during the surveillance 
    period. Surveillance 4.7.1.5.2 will identify a Mode 3 requirement to 
    perform a 10 second full closure test of the MSIVs in Mode 3 or 4. 
    Surveillance 4.7.1.5.3 will identify a Mode 4 requirement to perform 
    a 120 second full closure test of the MSIVs in Mode 4 when the RCS 
    temperature is greater than or equal to 320 degrees F. The 320 
    degrees F restriction on testing the valves is consistent with 
    recommendations from the valve manufacturer. Additionally, a 
    footnote is added to the LCO and the surveillance to identify that 
    the MSIVs are required to be closed and deactivated when the RCS 
    temperature is less than 320 degrees F. The footnote will eliminate 
    the potential to declare the MSIVs operable in the upper range of 
    Mode 4 and then allow the MSIVs to remain open during a cooldown 
    into the lower range of Mode 4 where they may not be able to meet 
    their required stroke time. The full closure test times are 
    consistent with the current MSIV surveillances and the partial 
    stroke testing is consistent with the Millstone Unit 3 Inservice 
    Pump and Valve Test Program.
        The other proposed changes to reword the Applicability and 
    Action statements of Technical Specification 3.7.1.5 and Bases 
    Section B3/4.7.1.5 are considered administrative changes.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270 NRC Deputy Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: June 30, 1997
        Description of amendment request: Technical Specifications 4.6.1.1, 
    3/4.6.1.2, and 3/4.6.1.3 require the testing of the containment to 
    verify leakage limits at a specified test pressure. The proposed 
    amendment would (1) modify the list of valves that can be opened in 
    Modes 1 through 4, (2) add a footnote on procedure controls, (3) remove 
    a footnote on Type A testing, and (4) make editorial changes to the 
    Technical Specifications and associated Bases sections.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 
    10CFR50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed revision does not involve [an] SHC because 
    the revision would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed changes to Technical Specification Surveillance 
    4.6.1.1.a include the adding ``or procedure control***'' and adding 
    footnote ``***''. The changes are requested since the Residual Heat 
    Removal System (RHR) valves, 3RHS*MV8701A/B and 3RHS*MV8702A/B, are 
    opened during cooldown and heatup in Mode 4. Allowing these 
    containment isolation valves to be opened is consistent with 
    Technical Specification 3.4.1.3, Reactor Coolant System - Hot 
    Shutdown, which allows the RHR system to be used in Mode 4. The 
    proposed changes to open the RHR system containment isolation 
    valves, under procedure control in Mode 4, do not change the way the 
    RHR system is operated or change the operator's response to an 
    accident in Mode 4.
        The proposed changes to Technical Specification Surveillance 
    4.6.1.1.a Footnote **, include the modification of the valves listed 
    in the footnote. Valves 3FPW-V661, 3FPW-V666, 3SAS-V875, 3SAS-V50, 
    3CCP-V886, 3CCP-V887 and 3CVS-V13 are being deleted and are local 
    manual containment isolation valves. Deleting these valves from the 
    list of valves that are allowed to be opened under administrative 
    control does not modify plant response to or mitigation strategy for 
    any accident. The valves being added, 3MSS*V885, 3MSS*V886, and 
    3MSS*V887, are in the steam lines to the steam-driven auxiliary 
    feedwater pump. These valves are opened to warm the steam lines 
    prior to testing the steam-driven auxiliary feedwater pump. These 
    valves were recently reclassified as containment isolation valves, 
    which resulted in the need to add them to the list of valves allowed 
    to be opened under administrative control. The administrative 
    controls include the appropriate considerations that when
    
    [[Page 40855]]
    
    required, containment integrity will be established consistent with 
    the assumptions in the design basis analyses.
        The proposed change to Technical Specification Surveillance 
    4.6.1.2.a will delete footnote ``*'' which referred to an exemption 
    granted by the NRC to permit the Type A test to be delayed until 
    RFO6 [refueling outage 6]. However, the current extended shutdown 
    has significantly delayed RFO6 and NNECO intends to perform the Type 
    A test during this midcycle shutdown. The deletion of the footnote 
    does not alter the operation of any system or the containment or 
    containment airlocks, as assumed for accident analyses.
        Additionally, Technical Specifications 4.6.1.1, 3/4.6.1.2 and 3/
    4.6.1.3 and Bases Sections 3/4.6.1.1, 3/4.6.1.2 and 3/4.6.1.3 are 
    reworded to provide clarity and consistency. These proposed changes 
    do not alter the operation of any system or the containment or 
    containment airlocks during accident analyses. Therefore, the 
    proposed revision does not involve a significant increase in the 
    probability or consequence of an accident previously evaluated.
        1. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to Technical Specifications 4.6.1.1, 3/
    4.6.1.2 and 3/4.6.1.3 and Bases Sections 3/4.6.1.1, 3/4.6.1.2 and 3/
    4.6.1.3 do not alter the operation of any system or the containment 
    or containment airlocks, during normal operation or as assumed in 
    accident analyses.
        Therefore, the proposed revision does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to Technical Specifications 4.6.1.1, 3/
    4.6.1.2 and 3/4.6.1.3 and Bases Sections 3/4.6.1.1, 3/4.6.1.2 and 3/
    4.6.1.3 do not alter the design, maintenance or function of any 
    system or the containment or the containment airlocks. Additionally, 
    the proposed changes do not alter the testing of any system or the 
    containment or containment airlocks, or alter any assumption used in 
    the accident analyses.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Deputy Director: Phillip F. McKee
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: May 14, 1997
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant, Unit Nos. 1 and 2 by revising Technical Specification (TS) 
    6.9.1.8.b.5 to replace reference WCAP-10266-P-A with WCAP-12945-P for 
    best estimate loss-of coolant accident (LOCA) analysis. The amendment 
    would also revise TS Bases 3/4.2.2 and 3/4.2.3 to change the emergency 
    core cooling system (ECCS) acceptance criteria limit to state that 
    there is a high level of probability that the ECCS acceptance criteria 
    limits are not exceeded. This is consistent with the best estimate LOCA 
    methodology.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change to use of the Best Estimate Loss of Coolant 
    Accident (LOCA) analysis methodology does not involve physical 
    alteration of any plant equipment or change in operating practice at 
    Diablo Canyon Power Plant (DCPP). Therefore, there will be no 
    increase in the probability of a LOCA. The consequences of a LOCA 
    are not being increased.
        The plant conditions assumed in the analysis are bounded by the 
    design conditions for all equipment in the plant. That is, it is 
    shown that the emergency core cooling system is designed so that its 
    calculated cooling performance conforms to the criteria contained in 
    10 CFR 50.46, paragraph b, and it meets the five criteria listed in 
    Section D. of this evaluation. No other accident is potentially 
    affected by this change.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change would not result in any physical alteration 
    to any plant system, and there would not be a change in the method 
    by which any safety related system performs its function. The 
    parameters assumed in the analysis are within the design limits of 
    existing plant equipment.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        It has been shown that the analytic technique used in the 
    analysis realistically describes the expected behavior of the DCPP 
    Units 1 and 2 reactor system during a postulated LOCA. Uncertainties 
    have been accounted for as required by 10 CFR 50.46. A sufficient 
    number of LOCAs with different break sizes, different locations, and 
    other variations in properties have been analyzed to provide 
    assurance that the most severe postulated LOCAs were calculated. It 
    has been shown by the analysis that there is a high level of 
    probability that all criteria contained in 10 CFR 50.46, paragraph 
    b, are met.
        Therefore the proposed changes do not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: May 15, 1997
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant (DCPP), Unit Nos. 1 and 2 to revise the surveillance 
    frequencies from at least once every 18 months to at least once per 
    refueling interval (nominally 24 months) including (1) reactor coolant 
    system total flow rate, (2) instrumentation for radiation monitoring, 
    (3) instrumentation and controls for remote shutdown, (4) 
    instrumentation for
    
    [[Page 40856]]
    
    accident monitoring, and (5) several miscellaneous TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed TS surveillance interval increases do not alter the 
    intent or method by which the inspections, tests, or verifications 
    are conducted, do not alter the way any structure, system, or 
    component functions, and do not change the manner in which the plant 
    is operated. The surveillance, maintenance, and operating histories 
    indicate that the equipment will continue to perform satisfactorily 
    with longer surveillance intervals. Few surveillance and maintenance 
    problems were identified. No problems have recurred, or are expected 
    to recur, following identification of root causes and implementation 
    of corrective actions.
        There was one time-related degradation mechanism identified that 
    could significantly degrade the performance of the evaluated 
    equipment during normal plant operation. Accumulation of corrosion 
    products and debris in the containment fan cooler unit (CFCU) 
    monitoring system drain lines could affect the use of the CFCU 
    drains as a backup to the containment gaseous monitor for RCS leak 
    detection. Primarily because CFCU drain line cleaning has been 
    instituted to reduce deposit buildup, and also because the CFCU 
    monitoring systems are used as backup and they are redundant by a 
    factor of five, it was evaluated that this time-related mechanism 
    will not significantly degrade the leak detection performance of the 
    CFCUs.
        All other potential time-related degradation mechanisms have 
    insignificant effects in the period of interest (24 months plus 25 
    percent allowance, or a maximum of 30 months). Instrument drift and 
    uncertainty analyses show that, while slight increases in instrument 
    drift can occur over a longer period, such increases are minimal and 
    remain within specified instrument accuracy and calibration 
    allowable values. In cases (pressurizer water level and RVLIS) where 
    greater than expected instrument drift has been found, design and 
    procedural changes have been implemented to improve the calibration 
    process and instrument performance. Based on the past performance of 
    the equipment, the probability or consequences of accidents 
    previously evaluated would not be significantly affected by the 
    proposed surveillance interval increases.
        The changes to commitments related to Bulletin 90-01 are 
    supported by the conclusions above, and otherwise do not alter the 
    intent or method by which the associated functions are tested, do 
    not alter the way any structure, system, or component functions, and 
    do not change the manner in which the plant is operated.
        The administrative changes to the Bases sections and to remove a 
    duplicate line do not alter the frequency, intent, or method by 
    which the associated functions are tested, do not alter the way any 
    structure, system, or component functions, and do not change the 
    manner in which the plant is operated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The surveillance and maintenance histories indicate that the 
    equipment will continue to effectively perform its design function 
    over the longer operating cycles. Additionally, the increased 
    surveillance intervals do not result in any physical modifications, 
    affect safety function performance or the manner in which the plant 
    is operated, or alter the intent or method by which surveillance 
    tests are performed. No problems have reoccurred following 
    identification of root causes and implementation of corrective 
    actions. Almost all identified potential time-related degradations, 
    including instrument drift, have insignificant effects in the period 
    of interest.
        The deposit buildup in the CFCU drain lines is time-related. 
    This was evaluated to not to be significant to the leak detection 
    function because the CFCUs have a redundancy factor of five (any one 
    of the five CFCUs can be used for the leak detection function) and 
    because the CFCU drain lines will be cleaned each refueling outage. 
    The proposed surveillance interval increases would not affect the 
    type or possibility of accidents.
        The changes to commitments related to Bulletin 90-01 are 
    supported by the conclusions above, and otherwise do not result in 
    any physical modifications, affect safety function performance or 
    the manner in which the plant is operated, or alter the intent or 
    method by which surveillance tests are performed.
        The administrative change to the Bases sections and to remove a 
    duplicate line do not result in any physical modifications, affect 
    safety function performance, or alter the frequency, intent, or 
    method by which surveillance tests are performed.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Evaluation of historical surveillance and maintenance data 
    indicates that there have been few problems experienced with the 
    evaluated equipment. There are no indications that potential 
    problems would be cycle-length dependent, with the exception of the 
    CFCU leak detection function, or that potential degradation would be 
    significant for the period of interest and, therefore, increasing 
    the surveillance interval will have negligible impact on safety. The 
    accumulation of corrosion products and debris in the CFCU drain 
    lines is cycle-length dependent, but has been evaluated to have 
    insignificant effect on its leak detection function. There is no 
    safety analysis impact since these changes will have no effect on 
    any safety limit, protection system setpoint, or limiting condition 
    for operation, and there are no hardware changes that would impact 
    existing safety analysis acceptance criteria. Safety margins are not 
    significantly impacted by surveillance intervals or by the slight 
    increases in instrument drift that may occur during the extended 
    interval.
        The changes to commitments related to Bulletin 90-01 are 
    supported by the conclusions above, and otherwise will have no 
    effect on any safety limit, protection system setpoint, or limiting 
    condition for operation, and there are no hardware changes that 
    would impact existing safety analysis acceptance criteria.
        The administrative change to the Bases sections and to remove a 
    duplicate line will have no effect on any safety limit, protection 
    system setpoint, or limiting condition for operation, and there are 
    no hardware changes that would impact existing safety analysis 
    acceptance criteria.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Pacific Gas and Electric Company, Docket No. 50-133, Humboldt Bay 
    Power Plant, Unit 3, Humboldt County, California
    
        Date of amendment request: December 9, 1996, as supplemented on 
    June 12, 1997.
        Description of amendment request: The proposed amendment would 
    revise the Humboldt Bay Power Plant (HBPP), Unit 3 Technical 
    Specifications (TSs) to incorporate the requirements of 10 CFR Part 50, 
    Appendix I, into the Radiological Effluent Technical Specifications 
    (RETS) and to relocate the controls and limitations on RETS and 
    radiological monitoring from the technical specifications to the 
    Offsite Dose Calculation Manual (ODCM) and the Process Control Program 
    (PCP). Additional minor administrative changes are proposed to make the 
    TSs on High Radiation Areas consistent with
    
    [[Page 40857]]
    
    the revised requirements in the new 10 CFR Part 20.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Operation of the facility in accordance with the proposed 
    amendment would not involve any increase in the probability or 
    consequences of an accident previously evaluated. This change places 
    new requirements in the Administrative Controls section of the 
    Technical Specifications to establish programs for the control of 
    radiological effluents and the conduct of radiological environmental 
    monitoring in the ODCM. The new Administrative Control requirements 
    for radiological effluents to be placed in the ODCM incorporate 10 
    CFR 50, Appendix I, limitations on dose to individual members of the 
    public that are much more restrictive than the current Technical 
    Specification limitations. The proposed changes do not involve 
    modifications to existing plant equipment, the addition of new 
    equipment, or operation of the plant in a different manner than 
    previously evaluated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability of consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Operation on the facility in accordance with the proposed 
    amendment will not create any new or different kind of accident from 
    any accident previously evaluated. As stated above, new programmatic 
    controls on radiological effluents and radiological environmental 
    monitoring are established in the Administrative Controls section of 
    the Technical Specifications. Additionally, this change is 
    administrative in nature; procedural details for radiological 
    effluents and radiological environmental monitoring are being 
    relocated to the ODCM and PCP consistent with the guidance provided 
    [by the NRC] in Generic Letter 89-01. The proposed changes do not 
    involve alterations to plant operating philosophy or methods, or in 
    changes to installed plant systems, structures, or components.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        Operation of the facility in accordance with the proposed 
    amendment would not involve any reduction in the margin of safety. 
    These changes do not involve a significant reduction in the margin 
    of safety. These changes do not involve a significant reduction in 
    the margin of safety. The changes will provide control over 
    radiological effluent releases, solid waste management, and 
    radiological environmental monitoring activities. Also, these 
    changes will increase the margin of safety for members of the public 
    by imposing additional controls to ensure that dose to members of 
    the public resulting from radioactive effluent releases will be 
    maintained ALARA.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Humboldt County Library, 636 F 
    Street, Eureka, California 95501
        Attorney for licensee: Christopher J. Warner, Esquire, Pacific Gas 
    and Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: Seymour H. Weiss
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket No. 50-321, Edwin I. Hatch 
    Nuclear Plant, Unit 1, Appling County, Georgia
    
        Date of amendment request: May 9, 1997
        Description of amendment request: The proposed amendment would 
    revise the Safety Limit Minimum Critical Power Ratio (SLMCPR) in 
    Technical Specification (TS) 2.1.1.2 to reflect results of a cycle-
    specific calculation performed for Unit 1 Operating Cycle 18 (expected 
    to commence November 1997).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed technical specification changes do not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        The derivation of the revised SLMCPR for Plant Hatch Unit 1 
    Cycle 18 for incorporation into the TS, and its use to determine 
    cycle-specific thermal limits, have been performed using NRC 
    approved methods. Additionally, interim implementing procedures that 
    incorporate cycle-specific parameters have been used which result in 
    a more restrictive value for SLMCPR. These calculations do not 
    change the method of operating the plantand have no effect on the 
    probability of an accident initiating event or transient.
        The basis of the MCPR Safety Limit is to ensure no mechanistic 
    fuel damage is calculated to occur if the limit is not violated. The 
    new SLMCPR preserves the existing margin to transition boiling and 
    the probability of fuel damage is not increased. Therefore, the 
    proposed changes do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes result only from a revised method of 
    analysis for the Unit 1 Cycle 18 core reload. These changes do not 
    involve any new method for operating the facility and do not involve 
    any facility modifications. No new initiating events or transients 
    result from these changes. Therefore, the proposed TS changes do not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety as defined in the TS bases will remain the 
    same. The new SLMCPR is calculated using NRC approved methods which 
    are in accordance with the current fuel design and licensing 
    criteria. Additionally, interim implementing procedures, which 
    incorporate cycle-specific parameters, have been used. The SLMCPR 
    remains high enough to ensure that greater than 99.9% of all fuel 
    rods in the core are expected to avoid transition boiling if the 
    limit is not violated, thereby preserving the fuel cladding 
    integrity.
        Therefore, the proposed TS changes do not involve a reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, 
    Edwin I. Hatch Nuclear Plant, Units 1 and 2, Appling County, 
    Georgia
    
        Date of amendment request: May 9, 1997
        Description of amendment request: The proposed amendments would 
    revise the operability requirements for the Rod Block Monitor system of 
    Technical Specification (TS) Table 3.3.2.1-1. The amendments would also
    
    [[Page 40858]]
    
    delete the requirements of TS Section 5.6.5 to report Rod Block Monitor 
    operability requirements in the cycle-specific Core Operating Limits 
    Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
    Southern Nuclear Operating Company has evaluated the proposed 
    changes to the Plant Hatch Units 1 and 2 Technical Specifications 
    in accordance with the criteria specified in 10 CFR 50.92 and has 
    determined that they do not involve a significant hazards 
    consideration because:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    since they are more restrictive than the existing requirements for 
    operation of the plant. These changes provide assurance that the Rod 
    Block Monitor system will remain operable when necessary to prevent 
    or mitigate the consequences of an anticipated operational 
    occurrence that could threaten the integrity of the fuel cladding 
    integrity. Since changes in RBM [Rod Block Monitor] operability 
    requirements do not involve any physical or functional modifications 
    in any plant system, structure or component, there will be no 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any previously evaluated because 
    they do not involve any changes in the plant configuration or in the 
    operation of any system, structure or component.
        3. The proposed changes do not reduce a margin of safety in the 
    plant because they impose more restrictive operability requirements 
    on the Rod Block Monitor system than those imposed by the existing 
    specifications. The changes are more restrictive in that they delete 
    the conditions under which the RBM is allowed to be bypassed at core 
    thermal power equal to or greater than 29% of rated power. These 
    more restrictive requirements ensure the RBM will not only prevent 
    fuel rods from under going transition boiling, they also prevent 
    fuel rods from exceeding 1% plastic strain (thereby avoiding fuel 
    cladding damage) during an RWE [rod withdrawal error] event.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Tennessee Valley Authority, Docket Nos. 50-260 and 50-296, Browns 
    Ferry Nuclear Plant, Units 2 and 3, Limestone County, Alabama
    
        Date of amendment request: June 19, 1997 (TS 391T)
        Description of amendment request: The proposed amendment extends 
    the allowed outage time for emergency diesel generators from 7 to 14 
    days on a one-time basis. This extension should permit completion of 
    extensive recommended maintenance within a single outage interval.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the ssue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The EDGs [emergency diesel generators] are designed as backup AC 
    [alternating current] power sources in the event of loss of off-site 
    power. The proposed AOT [allowed outage time] does not change the 
    conditions, operating configurations, or minimum amount of operating 
    equipment assumed in the safety analysis for accident mitigation. No 
    changes are proposed in the manner in which the EDGs provide plant 
    protection or which create new modes of plant operation. Also, the 
    TS [technical specification] change will improve the overall EDG 
    availability by allowing the consolidation of planned maintenance 
    outages and, hence, reducing the time period that each EDG will be 
    in an outage. Therefore, the proposed amendment does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not introduce any new modes of plant 
    operation or make physical changes to plant systems. Therefore, the 
    proposed one-time extension of the allowable AOT for EDGs does not 
    create the possibility of a new or different accident.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        BFN's [Browns Ferry Nuclear Plant's] emergency AC system is 
    designed with sufficient redundancy such that an EDG may be removed 
    from service for maintenance or testing. The remaining EDGs are 
    capable of carrying sufficient electrical loads to satisfy the UFSAR 
    [updated final safety analysis report] requirements for accident 
    mitigation or unit safe shutdown.
        Since the 12-year EDG PM [preventive maintenance] work activity 
    and vendor recommended PMs are required tasks which must be 
    performed, the proposed TS would reduce EDG unavailability since 
    multiple outages with resultant longer EDG outage times would not be 
    necessary to accomplish the planned maintenance activities.
        The proposed change does not impact the redundancy or 
    availability requirements of off-site power supplies or change the 
    ability of the plant to cope with station blackout events. The TS 
    change improves overall EDG availability. For these reasons, the 
    proposed amendment does not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET l0H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit 1, Ottawa County, Ohio
    
        Date of amendment request: June 24, 1997
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) Section 3/4.3.2.1, ``Safety 
    Features Actuation System Instrumentation,'' TS Section 3/4.6.1.7, 
    ``Containment Ventilation System,'' TS Section 3/4.6.3.1, ``Containment 
    Isolation Valves,'' and TS Section 3/4.9.4, ``Refueling Operations - 
    Containment Penetrations,'' and the associated TS Bases. Valve position 
    requirements would be added, and certain containment radiation monitor 
    requirements, valve isolation verification requirements, and 
    containment radiation monitor optional uses would be deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Toledo Edison has reviewed the proposed changes and determined 
    that a significant hazards consideration does not exist because 
    operation ofthe Davis-Besse Nuclear Power
    
    [[Page 40859]]
    
    Station (DBNPS), Unit No. 1, in accordance with this change would:
        1a Not involve a significant increase in the probability of an 
    accident previously evaluated because no accident initiators, 
    conditions, or assumptions are affected by the proposed changes.
        The proposed changes to the Technical Specifications and their 
    Bases ensure that during Modes 1 through 4 the Containment (CTMT) 
    purge and exhaust isolation valves are closed with control power 
    removed. Having these valves closed will not increase the 
    probability of an accident because these valves are not accident 
    initiators. They are used to mitigate the consequences of an 
    accident. The proposed changes require these valves to be maintained 
    in a closed position as required by design basis accident analysis.
        The removal of the Safety Features Actuation System (SFAS) 
    Radiation Monitors (RE's) and their associated SFAS Level 1 
    actuations does not affect any accident initiator, condition, or 
    assumption.
        During Modes 1 and 2 and partially in Mode 3, for design basis 
    accidents which require CTMT isolation, the high/high-high CTMT 
    pressure or low/low-low Reactor Coolant System (RCS) signals provide 
    CTMT isolation and isolation and actuation of those components 
    presently actuated by an SFAS Level 1 High Radiation signal. During 
    Mode 3, when the RCS pressure is below 1800 psig, the low RCS 
    pressure trip may be manually bypassed, and when the RCS pressure is 
    below 600 psig, the low-low pressure trip may be manually bypassed. 
    During the short period of time that these bypasses are activated in 
    Mode 3, CTMT isolation is only automatically initiated by the CTMT 
    high/high-high pressure trips. Manual SFAS actuation is also 
    available, including Modes 1 through 4. Removing the SFAS RE's does 
    not affect the operation of the SFAS Levels 2-4 actuation since 
    these are based only on containment pressure and RCS pressure. 
    Therefore, the assumption of CTMT isolation following design basis 
    accidents is maintained.
        The SFAS is not required in Mode 5. During Mode 6, the SFAS RE's 
    and their associated SFAS Level 1 actuation are not credited during 
    a fuel handling accident inside CTMT. The analysis for a fuel 
    handling accident inside CTMT assumes that there is no isolation of 
    CTMT. The probability of a fuel handling accident is not affected by 
    these changes.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because the proposed changes do not 
    change the source term, CTMT isolation, or allowable releases.
        The proposed changes to the Technical Specifications and their 
    Bases ensure that during Modes 1 through 4, the CTMT purge and 
    exhaust isolation valves are closed with control power removed.
        Having these valves closed and their control power removed 
    ensures that the valves are in and will remain in, the proper 
    position for CTMT isolation during and following design basis 
    accidents. Also, during Modes 1 and 2 and partially in Mode 3, SFAS 
    actuation on high/high-high CTMT pressure or low/low-low RCS 
    pressure provides for diverse CTMT isolation. As noted above, during 
    Mode 3, when the RCS pressure is below 1800 psig, the low RCS 
    pressure trip may be manually bypassed, and when the RCS pressure is 
    below 600 psig, the low-low pressure trip may be manually bypassed. 
    During the short period of time that these bypasses are activated in 
    Mode 3, CTMT isolation is only automatically initiated by the CTMT 
    high/high-high pressure trips. In addition, manual SFAS actuation is 
    also available, including during Modes 1 through 4. Therefore, 
    removal of the SFAS RE's and their actuation signal does not prevent 
    CTMT isolation.
        The SFAS RE's and automatic isolation of the CTMT purge and 
    exhaust isolation valves during a fuel handling accident is not 
    required because the CTMT purge and exhaust isolation system, 
    including the associated noble gas monitor, with operator action, 
    can provide the necessary actions to mitigate a fuel handling 
    accident inside CTMT, assuming the purge and exhaust valves are 
    open. Therefore, removing the SFAS RE's and their actuation signal 
    will not increase the consequences of an accident because CTMT 
    closure is ensured. Further, it is noted that CTMT isolation is not 
    assumed in the accident analysis for the fuel handling accident.
        The Containment Radiation-High trip feature is not credited for 
    any DBNPS Updated Safety Analysis Report (USAR) accident analysis, 
    therefore the proposed removal of this feature will not impact 
    radiological consequences of such accidents.
        2. Not create the possibility of a new or different kind of 
    accident from any accident previously evaluated because no new 
    accident initiators or assumptions are introduced by the proposed 
    changes.
        As stated above, the CTMT purge and exhaust isolation valves, 
    the SFAS RE's, and SFAS actuation are not accident initiators. 
    Maintaining the CTMT purge and exhaust isolation valves closed and 
    control power removed ensures that the design basis assumption of 
    CTMT isolation is maintained. Also, since SFAS Levels 2-4 actuation, 
    as applicable, on high/high-high CTMT pressure or low/low-low RCS 
    pressure or by manual actuation provides the required diversity of 
    sensing parameters and isolation of CTMT, the SFAS RE's and their 
    associated automatic isolation of the CTMT purge and exhaust 
    isolation valves is not required during Modes 1 through 4. 
    Therefore, no new or different kind of accident will be introduced.
        3. Not involve a significant reduction in a margin of safety 
    because the proposed changes maintain a redundant and diverse CTMT 
    isolation capability following design basis accidents. Under TS 3/
    4.3.2, diversity in achieving CTMT isolation by means of a high/
    high-high CTMT pressure or low/low-low RCS pressure SFAS actuation 
    will be maintained during Modes 1 through 3 (except during brief 
    periods of bypass in Mode 3), and the redundancy of the SFAS sensor 
    instrumentation channels and actuation channels themselves will be 
    maintained. During Modes 1 through 4 the manual actuation capability 
    of SFAS will be maintained. During Modes 1 through 4, control room 
    indication of normal and accident range radiation monitoring will be 
    maintained in accordance with TS 3/4.3.3.1 and 3/4.4.6.1.
        Under TS 3/4.6.1.7, requiring the CTMT purge and exhaust 
    isolation valves to be closed with control power removed, and 
    requiring an open CTMT purge and exhaust isolation valve to be 
    closed with control power removed within 24 hours is more 
    restrictive than the current Technical Specifications or ``The 
    Improved Standard Technical Specifications for Babcock and Wilcox 
    Plants,'' NUREG-1430, Revision 1. Under TS 3/4.9.4, the existing 
    requirements already allow for the SFAS-initiated closure of the 
    CTMT purge and exhaust isolation valves to be unavailable and the 
    CTMT purge and exhaust system noble gas monitor used as an 
    alternative means of achieving CTMT isolation. Further, it is noted 
    that CTMT isolation is not credited in the accident analysis for the 
    fuel handling accident. Therefore, these proposed changes do not 
    significantly reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, OH 43606
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
    Date of application request: April 24, 1997, as supplemented by 
    letters dated June 6, 1997, and June 27, 1997.
    
        Description of amendment request: The amendment would revise 
    Section 6.0 of the Technical Specifications to change the title 
    ``Senior Vice President, Nuclear'' to ``Vice President and Chief 
    Nuclear Officer.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This proposed change does not involve any hardware or design 
    changes, plant procedures, or administrative changes, other than a 
    revision of title designation in documentation. Within the Union 
    Electric
    
    [[Page 40860]]
    
    organizational structure, the departments reporting to the former 
    Senior Vice-President, Nuclear now report to the Vice President and 
    Chief Nuclear Officer. The position of Vice-President and Chief 
    Nuclear Officer now reports to the President & Chief Executive 
    Officer of Union Electric, which is the same management level of 
    reporting as the previous title, Senior Vice-President, Nuclear. 
    This change has no impact on the probability or consequences of 
    accidents previously evaluated in the Final Safety Report (FSAR).
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This proposed change does not involve any hardware or design 
    changes, plant procedures, or administrative changes, other than a 
    revision of title designation in documentation. Within the Union 
    Electric organizational structure, the departments reporting to the 
    former Senior Vice-President, Nuclear now report to the Vice 
    President and Chief Nuclear Officer. The position of Vice-President 
    and Chief Nuclear Officer now reports to the President & Chief 
    Executive Officer of Union Electric, which is the same management 
    level of reporting as the previous title, Senior Vice-President, 
    Nuclear. No new or different kind of accident is introduced by this 
    purely administrative change to revise documentation to reflect 
    current organizational titles.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The safety margins of the Technical Specifications are based on 
    the actual plant design and are unaffected by this purely 
    administrative change. This change merely updates the Technical 
    Specifications to reflect the current organizational title for 
    senior management of the Callaway Plant, and within the 
    organizational structure of Union Electric. This change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: May 14, 1997
        Description of amendment request: The proposed change will provide 
    clarification to the testing and inspection requirements that each of 
    the turbine control valves be cycled and movement verified through at 
    least one complete cycle from the running position and revise the 
    current wording in Surveillance Requirement 4.7.1.7.2.a for both units 
    to clarify the testing and inspection methodology of the turbine 
    control valves. Additionally, Technical Specification Bases Section 3/
    4.7.1.7 will be revised to clarify the testing requirements for the 
    turbine governor control valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of the North Anna Power Station in 
    accordance with the proposed Technical Specifications changes will 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        No new or unique accident precursors are introduced by these 
    changes in surveillance requirements. The clarification for the 
    turbine control valve testing and inspections do not change
        the design, operation, or failure modes of the valves and other 
    components in the turbine overspeed protection system.
        The verification of the operability of the turbine control 
    valves will continue to provide adequate assurance that the turbine 
    overspeed protection system will operate as designed, if needed. 
    Therefore, these changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previous[ly] evaluated.
        Since the implementation of the proposed change to the 
    surveillance requirements is to clarify the wording only, operation 
    of the facilities with these proposed Technical Specifications does 
    not create the possibility for any new or different kind of accident 
    which has not already been evaluated in the Updated Final Safety 
    Analysis Report (UFSAR).
        The proposed wording changes to the Technical Specifications 
    will not result in any physical alteration to any plant system, nor 
    would there be a change in the method by which any safety-related 
    system performs its function. The design and operation of the 
    turbine overspeed protection and turbine control systems are not 
    being changed. The proposed change merely represents a clarification 
    to more specifically state current test requirements and test 
    practice.
        These changes do not change the design, operation, or failure 
    modes of the valves and other components of the turbine overspeed 
    protection system. Therefore, the proposed change does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes would not reduce the margin of safety as 
    defined in the basis for any Technical Specifications. The design 
    and operation of the turbine overspeed protection and turbine 
    control systems are not being changed and the operability of the 
    turbine control valves are being demonstrated in the same manner. In 
    addition, the results of the accident analyses which are documented 
    in the UFSAR continue to bound operation under the proposed changes, 
    so that there is no safety margin reduction. Therefore, the proposed 
    change does not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219
        NRC Project Director: Gordon E. Edison, Acting
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 3, 1997
        Description of amendment request: This license amendment request 
    revises Technical Specification Section 5.3.1, Fuel Assemblies, to 
    allow the use of an alternate zirconium based fuel cladding material, 
    ZIRLO. Wolf Creek Nuclear Operating Corporation (WCNOC) is planning to 
    insert Westinghouse fuel assemblies containing ZIRLO fuel rod cladding 
    during the ninth refueling outage, which is currently scheduled to 
    begin in October 1997. This request proposes to incorporate additional 
    information, associated with the requested change, into Technical 
    Specification 6.9.1.9, ``CORE OPERATING LIMITS REPORT (COLR).'' This 
    revised submittal supersedes the staff's proposed no significant 
    hazards consideration determination evaluation for the requested 
    changes that were published on April 23, 1997 (62 FR 19839).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the
    
    [[Page 40861]]
    
    issue of no significant hazards consideration, which is presented 
    below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The methodologies used in the accident analysis remain 
    unchanged. The proposed changes do not change or alter the design 
    assumptions for the systems or components used to mitigate the 
    consequences of an accident. Use of ZIRLO fuel cladding does not 
    adversely affect fuel performance or impact nuclear design 
    methodology. Therefore accident analyses are not impacted.
        The operating limits will not be changed and the analysis 
    methods to demonstrate operation within the limits will remain in 
    accordance with NRC approved methodologies. Other than the changes 
    to the fuel assemblies, there are no physical changes to the plant 
    associated with this technical specification change. A safety 
    analysis will continue to be performed for each cycle to demonstrate 
    compliance with all fuel safety design basis.
        VANTAGE 5H with IFMs fuel assemblies with ZIRLO clad fuel rods 
    meet the same fuel assembly and fuel rod design bases as other 
    VANTAGE 5H with IFMs fuel assemblies. In addition, the 10 CFR 50.46 
    criteria are applied to the ZIRLO clad rods. The use of these fuel 
    assemblies will not result in a change to the reload design and 
    safety analysis limits. The clad material is similar in chemical 
    composition and has similar physical and mechanical properties as 
    Zircaloy-4. Thus, the cladding integrity is maintained and the 
    structural integrity of the fuel assembly is not affected. ZIRLO 
    cladding improves corrosion performance and dimensional stability. 
    No concerns have been identified with respect to the use of an 
    assembly containing a combination of Zircaloy-4 and ZIRLO clad fuel 
    rods. Since the dose predictions in the safety analyses are not 
    sensitive to fuel rod cladding material, the radiological 
    consequences of accidents previously evaluated in the safety 
    analysis remain valid.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident or 
    malfunction of equipment important to safety previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        VANTAGE 5H with IFMs fuel assemblies with ZIRLO clad fuel rods 
    satisfy the same design bases as those used for other VANTAGE 5H 
    with IFMs fuel assemblies. All design and performance criteria 
    continue to be met and no new failure mechanisms have been 
    identified. Since the original design criteria are met, the ZIRLO 
    clad fuel rods will not be an initiator for any new
        accident or malfunction of equipment important to safety. The 
    ZIRLO cladding material offers improved corrosion resistance and 
    structural integrity.
        The proposed changes do not affect the design or operation of 
    any system or component in the plant. The safety functions of the 
    related structures, systems or components are not changed in any 
    manner, nor is the reliability of any structure, system or component 
    reduced. The changes do not affect the manner by which the facility 
    is operated and do not change any facility design feature, structure 
    or system. No new or different type of equipment will be installed. 
    Since there is no change to the facility or operating procedures, 
    and the safety functions and reliability of structures, systems and 
    components are not affected, the proposed changes do not create the 
    possibility of a new or different kind of accident or malfunction of 
    equipment important to safety from any accident or malfunction of 
    equipment important to safety previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Use of ZIRLO cladding material does not change the VANTAGE 5H 
    with IFMs reload design and safety limits. The use of these fuel 
    assemblies will take into consideration the normal core operating 
    conditions allowed in the Technical Specifications. For each cycle 
    reload core, the fuel assemblies will be evaluated using NRC 
    approved reload design methods, including consideration of the core 
    physics analysis peaking factors and core average linear heat rate 
    effects.
        The use of Zircaloy-4, ZIRLO or stainless steel filler rods in 
    fuel assemblies will not involve a significant reduction in the 
    margin of safety because analyses using NRC approved methodologies 
    will be performed for each configuration to demonstrate continued 
    operation within the limits that assure acceptable plant response to 
    accidents and transients. These analyses will be performed using NRC 
    approved methods that have been approved for application to the fuel 
    configuration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.Local 
    Public Document Room locations: Emporia State University, William Allen 
    White Library, 1200 Commercial Street, Emporia, Kansas 66801 and 
    Washburn University School of Law Library, Topeka, Kansas 66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 3, 1997
        Description of amendment request: This license amendment request 
    revises Definition 1.9, ``CORE ALTERATION.'' This change will more 
    clearly define the types of components that constitute a core 
    alteration when moved.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The probability of occurrence of a previously evaluated accident 
    is not increased because this change to the definition of core 
    alteration does not introduce any new potential accident initiating 
    conditions. The proposed change will not affect any previously 
    evaluated accident scenario. This proposed change will not affect 
    any currently approved refueling-related operating activities. The 
    consequences of an accident previously evaluated is not increased 
    because the ability of containment to restrict the release of any 
    fission product radioactivity to the environment will not be 
    degraded by this change.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not affect any previously evaluated 
    accident scenarios, nor does it create any new accident scenarios. 
    The proposed change does not alter any of the currently-approved 
    refueling operation activities, nor does it create any new refueling 
    operating activities.
        Therefore, this proposed change will not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        WCGS Technical Specification 3/4.9.1, Boron Concentration, 
    specifies that Keff will be maintained equal to or less 
    than 0.95 during Operating Mode 6 with fuel in the vessel and the 
    vessel head removed. The proposed change in the definition of core 
    alteration will allow ``non-core'' components, such as cameras, 
    lights, fuel inspection tools, etc., to be moved or manipulated in 
    the vessel, with fuel in the vessel and the vessel head removed, 
    without constituting a core alteration. This is acceptable because 
    these types of components will have no effect on core reactivity, 
    and will not affect reactor coolant system boron concentrations. 
    Therefore, operations using these types of components will not 
    adversely affect Keff or the shutdown margin. Reactor 
    subcriticality status is continuously monitored in the control room 
    during Operating Mode 6, as specified in WCGS Technical 
    Specification 3/4.9.2, Instrumentation.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff
    
    [[Page 40862]]
    
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 3, 1997
        Description of amendment request: This license amendment request 
    revises Surveillance Requirements 4.3.1.2 and 4.3.2.2 of Technical 
    Specification (TS) 3/4.3.1, ``Reactor Trip System Instrumentation'' and 
    TS 3/4.3.2, ``Engineered Safety Features Actuation System 
    Instrumentation'' and associated Bases to indicate that the total 
    response time will be determined based on the results of WCAP-13632-P-A 
    Revision 2, ``Elimination of Pressure Sensor Response Time Testing 
    Requirements.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The same RTS [Reactor Trip System] and ESFAS [Engineered Safety 
    Features Actuation System] instrumentation is being used. The time 
    response allocations/modeling assumptions in the Updated Safety 
    Analysis Report Chapter 15 analyses are still the same, only the 
    method of verifying time response is changed. The proposed change 
    will not modify any system interface and could not increase the 
    likelihood of an accident since these events are independent of this 
    change. The proposed activity will not change, degrade or prevent 
    actions or alter any assumptions previously made in evaluating the 
    radiological consequences of an accident described in the USAR. The 
    proposed change will not affect the probability of any event 
    initiators, nor will the proposed change affect the ability of any 
    safety-related equipment to perform its intended function. There 
    will be no degradation in the performance of, nor an increase in the 
    number of challenges imposed on safety-related equipment assumed to 
    function during an accident situation. Therefore, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There are no hardware changes, nor are there any changes in the 
    method by which any safety-related plant system performs its safety 
    function. The change will not alter the normal method of plant 
    operation. No transmitter performance requirements will be affected. 
    This change does not alter the performance of the pressure and 
    differential pressure transmitters used in the plant protection 
    systems. All sensors will still have response times verified by test 
    before placing the sensors in operational service, and after any 
    maintenance that could affect response time. Changing the method of 
    periodically verifying instrument response for certain sensors 
    (assuring equipment operability) from time response testing to 
    calibration and channel checks will not create any new accident 
    initiators or scenarios. Periodic surveillance of these instruments 
    will detect significant degradation in the sensor response 
    characteristic. No new transient precursors, failure mechanisms, or 
    limiting single failures are introduced as a result of this change. 
    Therefore, the proposed change does not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not affect the acceptance criteria for 
    any analyzed event. This change does not affect the total system 
    response time assumed in the safety analysis. The periodic system 
    response time verification method for selected pressure and 
    differential pressure sensors is modified to allow use of actual 
    test data or engineering data. The method of verification still 
    provides assurance that the total system response is within
        that defined in the safety analysis, since calibration tests 
    will detect any degradation which might significantly affect sensor 
    response time. There will be no effect on the manner in which safety 
    limits or limiting safety system settings are determined, nor will 
    there be any effect on those plant systems necessary to assure the 
    accomplishment of protection functions. There will be no impact on 
    any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: January 27, 1997, as 
    supplemented May 16, 1997.
        Brief description of amendment: The amendment revised the Technical 
    Specifications to permit control rod misalignment of plus or minus 18 
    steps when the core power is less than or equal to 85% of rated thermal 
    power (RTP) and plus or minus 12 steps above 85% RTP.
        Date of publication of individual notice in Federal Register: June 
    19, 1997 (62 FR 33445)
        Expiration date of individual notice: July 21, 1997
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in
    
    [[Page 40863]]
    
    10 CFR Chapter I, which are set forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
    Date of application for amendments: January 20, 1997
    
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) 3.6.3, ``Containment Isolation Valves,'' to reflect 
    modifications associated with steam generator replacement for Unit 1 of 
    each station. TS Table 3.6-1, ``Containment Isolation Valves,'' will be 
    modified to reflect the deletion of feedwater bypass valves and 
    reassignment of certain isolation valves to different containment 
    penetrations. TS pages for Unit 2 of each station are affected because 
    Units 1 and 2 share common TS pages.
        Date of issuance: : July 10, 1997Effective date: Immediately, to be 
    implemented within 30 days.
        Amendment Nos.: 91, 90, 84, and 83
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: March 12, 1997 (62 FR 
    11489). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 10, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481
    
    Commonwealth Edison Company, Docket No. 50-010, Dresden Nuclear 
    Generating Station, Unit 1, Grundy County, Illinois
    
        Date of application for amendment: October 23, 1996, as 
    supplemented November 25, 1996, and June 5, 1997.
        Brief description of amendment: The amendment replaces the Appendix 
    A Technical Specifications of License DPR-2 in their entirety. The 
    amendment revises the Dresden 1 Technical Specifications (TS) to the 
    same format as the Dresden Nuclear Power Station, Units 2 and 3 
    (Dresden 2/3) Technical Specification Upgrade Program (TSUP).
        Date of issuance: July 8, 1997
        Effective date: July 8, 1997
        Amendment No.: 39
        Facility Operating License No. DPR-2: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4343). The November 25, 1996, and June 5, 1997, submittals provided 
    additional clarifying information that did not change the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated July 8, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: January 20, 1997
        Brief description of amendments: The amendments revise the 
    Technical Specifications for various instruments which have alarm or 
    indication functions. The amendments relocate surveillance requirements 
    for selected instrumentation from Technical Specifications to licensee 
    controlled documents or replace selected surveillance requirements with 
    those more appropriate to the associated LCOs. In addition, the 
    amendments add an action statement related to the automatic 
    depressurization system accumulator backup compressed gas system and 
    delete action statements related to suppression chamber water level 
    instrumentation.
        Date of issuance: July 16, 1997
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 118 and 103
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8795) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 16, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: August 15, 1996, as supplemented by 
    letters dated October 31, 1996, and May 29, 1997.
        Brief description of amendments: The amendments removed a 
    requirement for performance of a surveillance incorporating a high 
    toxic gas test signal.
        Date of issuance: July 17, 1997
        Effective date: July 17, 1997, to be implemented within 30 days.
        Amendment Nos.: Unit 1 - Amendment No. 88; Unit 2 - Amendment No. 
    75
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 25, 1996 (61 
    FR 50344) The additional information contained in the supplemental 
    letters dated October 31, 1996, and May 29, 1997, were clarifying in 
    nature and thus, within the scope of the initial notice and did not 
    affect the staff's proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 17, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior
    
    [[Page 40864]]
    
    College, J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 
    77488
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 14, 1997
        Brief description of amendment: Technical Specification 3.4.9.3 
    requires, in part, that two residual heat removal suction relief valves 
    be operable to protect the reactor coolant system from 
    overpressurization when any reactor coolant system cold leg is less 
    than 350 degrees. The amendment revises the setpoint of the residual 
    heat removal suction relief valves.
        Date of issuance: July 10, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 143
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 4, 1997 (62 FR 
    30634) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 10, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: June 10, 1996, as supplemented 
    July 25, 1996
        Brief description of amendments: These amendments change the 
    differential temperature Technical Specifications allowable values and 
    trip setpoints for the reactor water cleanup system penetration room 
    steam leak detection function.
        Date of issuance: June 26, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 166 and 140
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64389) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 26, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: December 23, 1996, as 
    supplemented February 26, 1997, May 12, 1997, June 16, 1997, and July 
    2, 1997 and July 11, 1997.
        Brief description of amendment: The amendment changes the Technical 
    Specifications to allow the use of VANTAGE+ fuel for cycle 10.
        Date of issuance: July 15, 1997
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 175
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6578). The February 26, 1997, May 12, 1997, and June 16, 1997, July 
    2, 1997 and July 11, 1997, letters provided information that did not 
    change the initial no proposed significant hazards consideration 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 15, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: March 31, 1997
        Brief description of amendment: This amendment changes Hope Creek 
    Technical Specification Section 3.6.5.3.2, ``Filtration, Recirculation 
    and Ventilation System (FRVS),'' to provide an appropriate Limiting 
    Condition for Operation and ACTION Statement that reflects the design 
    basis for the FRVS.
        Date of issuance: July 9, 1997
        Effective date: July 9, 1997, to be implemented within 60 days
        Amendment No.: 99
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 21, 1997 (62 FR 
    27798) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 9, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Pennsville Public Library, 
    190 S. Broadway, Pennsville, NJ 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: June 18, 1996, as supplemented 
    August 19, 1996, April 28, 1997, and June 11, 1997
        Brief description of amendments: The amendments change Technical 
    Specification (TS) 5.2.2, ``Design Pressure and Temperature,'' by 
    adding design parameters for Main Steam Line Break (MSLB). The MSLB 
    analysis results in a higher containment air temperature than the value 
    that was in TS 5.2.2 prior to the issuance of these amendments.
        Date of issuance: July 17, 1997
        Effective date: July 17, 1997
        Amendment Nos.: 198 and 181
        Facility Operating License Nos. DPR-70 and DPR-75: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 17, 1996 (61 FR 
    37302) The supplemental letters did not change the original no 
    significant hazards consideration determination nor the Federal 
    Register notice. The Commission's related evaluation of the amendments 
    is contained in a Safety Evaluation dated July 17, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: August 30, 1996 (TS 380)
        Brief description of amendment: The amendments remove License 
    Condition 2.C.(3) regarding thermal water quality limits.
        Date of issuance: July 8, 1997
        Effective Date: Effective as of the date of issuance.
        Amendment Nos.: 232, 248 and 208
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revise the license.
        Date of initial notice in Federal Register: September 25, 1996 (61 
    FR
    
    [[Page 40865]]
    
    50347) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 8, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Athens Public library, South 
    Street, Athens, Alabama 35611
    
    Tenessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: August 22, 1996 (TS 96-08)
        Brief description of amendments: The amendments change the 
    Technical Specifications (TS) by eliminating the emergency diesel 
    generator accelerated testing and special reporting requirements TS 
    4.8.1.1.2.a in accordance with NRC Generic Letter 94-01.
        Date of issuance: : July 14, 1997
        Effective date: July 14, 1997
        Amendment Nos.: 226 and 217
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the TS.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52969) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 14, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: December 17, 1996
        Brief description of amendments: The proposed changes will allow 
    one of the two service water loops to be isolated from the component 
    cooling water heat exchangers (CCHXs) during power operation in order 
    to refurbish sections of the isolated service water headers. The 
    proposed temporary changes will be valid for two periods of up to 35 
    days each for implementation of the service water upgrades associated 
    with the repair of the sections of the 24-inch service water supply and 
    return piping to/from the CCHXs.
        Date of issuance: July 17, 1997
        Effective date: July 17, 1997
        Amendment Nos.: 205 and 186
        Facility Operating License Nos. NPF-4 and NPF-7:. These amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6580) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 17, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498Virginia Electric and Power Company, et al., Docket 
    Nos. 50-280 and 50-281, Surry Power Station, Units 1 and 2, Surry 
    County, Virginia
        Date of application for amendments: November 26, 1997
        Brief description of amendments: These amendments revise the 
    Technical Specifications (TSs) to eliminate the records retention 
    requirements from Section 6.5 of the TSs. The relocation of those 
    requirements to the Operational Quality Assurance program, contained in 
    the Final Safety Analysis Report, has been completed.
        Date of issuance: July 15, 1997
        Effective date: July 15, 1997
        Amendment Nos.: 211 and 211
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    change the Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14472) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 15, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-280 and 
    50-281, Surry Power Station, Units 1 and 2, Surry County, Virginia
    
        Date of application for amendments: February 3, 1997, and March 18, 
    1997
        Brief description of amendments: These amendments revise the 
    Technical Specifications to eliminate the inconsistency between the 
    current approved Inservice Inspection Program and ASME Code (1989 
    Edition) and the Surry Technical Specifications (TS) as required by 10 
    CFR 50.55a(g)95)(ii).
        Date of issuance: July 15, 1997
        Effective date: July 15, 1997
        Amendment Nos.: 212 and 212
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    change the Technical Specifications.
        Date of initial notice in Federal Register: April 9, 1997 (62 FR 
    17242) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 15, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: May 20, 1997, as supplemented by 
    letters dated June 6, 1997, and July 3, 1997. Additional information 
    was also received by letters dated June 12, June 20, and June 25, 1997.
        Brief description of amendment: The amendment modifies the 
    Technical Specifications (TS) for the minimum critical power ratio 
    (MCPR) safety limit in TS 2.1.1.2 for ATRIUM 9X9 fuel. This change is 
    effective for Cycle 13 operation only.
        Date of issuance: July 3, 1997
        Effective date: July 3, 1997, to be implemented within 30 days from 
    the date of issuance.
        Amendment No.: 151
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications and operating license.
        Date of initial notice in Federal Register: May 29, 1997 (62 FR 
    29160). The June 12, June 20, June 25, and July 3, 1997, submittals 
    provided clarifying information which did not affect the initial no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated July 3, 1997. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: September 30, 1996 (TSCR-192), 
    as supplemented on November 26 and December 12, 1996, February 13, 
    March 5, April 2, April 16, May 9, June 3, June 13 (two letters), and 
    June 25, 1997
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) 15.3.3, ``Emergency Core Cooling System, Auxiliary 
    Cooling Systems, Air Recirculation Fan Coolers, and Containment 
    Spray,'' to incorporate allowed outage times similar to those contained 
    in NUREG-1431, Revision 1, ``Westinghouse Owner's Group Improved 
    Standard Technical
    
    [[Page 40866]]
    
    Specifications,'' and modify the operability requirements for the 
    service water and component cooling water systems. TS 15.3.7, 
    ``Auxiliary Electrical Systems,'' was revised to reflect the changes to 
    the service water system operability requirements. These changes ensure 
    that TS requirements are the ``lowest functional capability or 
    performance levels of equipment required for safe operation of the 
    facility,'' as defined in 10 CFR 50.36(c)(2), ``Limiting Conditions for 
    Operation.'' Additionally, the amendments change TS 15.3.12, ``Control 
    Room Emergency Filtration,'' to revise charcoal filtration efficiencies 
    and to include a specific testing standard, and TS 15.5.2, 
    ``Containment,'' to revise the design heat removal capability of the 
    containment fan coolers.
        Date of issuance: July 9, 1997
        Effective date: July 9, 1997, with full implementation prior to 
    restart of Unit 2 and Unit 1 and no later 45 days from the date of 
    issuance. Implementation includes incorporating changes to TS 
    requirements for the service water system, component cooling water 
    systems, and control room ventilating system as detailed in an 
    application dated September 30, 1996, as supplemented on November 26 
    and December 12, 1996, February 13, March 5, April 2, April 16, May 9, 
    June 3, June 13 (two), and June 25, 1997, and evaluated in the staff's 
    safety evaluation dated July 9, 1997. These amendments are authorized 
    contingent on compliance to commitments provided by the licensee, to 
    meet the dose limits associated with Title 10, Code of Federal 
    Regulations, Part 50, Appendix A, General Design Criterion (GDC) 19 by: 
    (1) submitting a license amendment application including supporting 
    analyses and evaluations by February 27, 1998, that contains the 
    proposed methods for compliance with GDC 19 dose limits under accident 
    conditions based on system design and without reliance on the use of 
    potassium iodide and/or self contained breathing apparatus, and (2) 
    implementing the proposed changes within 2 years of the date that NRC 
    approval for the proposed license amendment is granted. Additionally, 
    these amendments are authorized contingent on compliance to commitments 
    provided by the licensee, to operate Point Beach Nuclear Plant in 
    accordance with its service water system analyses and approved 
    procedures. Specifically, each unit will utilize only one component 
    cooling water (CCW) heat exchanger until such time that analyses are 
    completed and the service water system reconfigured as necessary to 
    allow operation of one or both units with two heat exchangers in 
    service. If two CCW heat exchangers are required in one or both units 
    for maintaining acceptable CCW temperature prior to completion of 
    necessary analyses to allow operation in the required configuration, 
    the service water system will be considered in an unanalyzed condition, 
    declared inoperable and action taken as specified by TS 15.3.0.B except 
    for short periods of time as necessary to effect procedurally 
    controlled changes in system lineups and unit operating conditions.
        Amendment Nos.: 174 and 178
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Licenses and Technical Specifications. Public comments 
    requested as to proposed no significant hazards considerations (NSHC): 
    Yes (61 FR 58905 dated November 19, 1996; 62 FR 17244 dated April 9, 
    1997; and 62 FR 31636 dated June 10, 1997). No comments have been 
    received. The June 10, 1997, notice also provided for an opportunity to 
    request a hearing by July 10, 1997, but indicated that if the 
    Commission makes a final NSHC determination, any such hearing would 
    take place after issuance of the amendments. The June 13 and June 25, 
    1997, submittals provided clarifying information within the scope of 
    the application and did not affect the staff's previous no significant 
    hazards considerations determinations. The Commission's related 
    evaluation of the amendments, finding of exigent circumstances, and 
    final determination of no significant hazards considerations are 
    contained in a Safety Evaluation dated July 9, 1997.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        Local Public Document Room location: The Lester Public Library 1001 
    Adams Street, Two Rivers, WI 54241
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: April 23, 1997
        Brief description of amendment: This amendment allows the service 
    air and breathing air containment penetrations to remain open under 
    administrative control during periods of core alterations or movement 
    of irradiated fuel inside containment.
        Date of issuance: July 11, 1997
        Effective date: July 11, 1997, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 107
        Facility Operating License No. NPF-42: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 4, 1997 (62 FR 
    30648) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 11, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of
    
    [[Page 40867]]
    
    telephone comments, the comments have been recorded or transcribed as 
    appropriate and the licensee has been informed of the public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By August 29, 1997, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. A copy of the petition should also be sent to the Office of the 
    General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained
    
    [[Page 40868]]
    
    absent a determination by the Commission, the presiding officer or the 
    Atomic Safety and Licensing Board that the petition and/or request 
    should be granted based upon a balancing of the factors specified in 10 
    CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: July 10, 1997
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications by deleting the requirements of Surveillance 
    Requirements (SR) 4.8.1.1.2.h.2 for the diesel fuel oil system. This 
    change will result in testing of the diesel fuel oil system in 
    accordance with ASME Code Section XI requirements.
        Date of issuance: July 11, 1997
        Effective date: July 11, 1997, with full implementation within 30 
    days.
        Amendment No: 132
        Facility Operating License No. NPF-38: Amendment revises the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated July 11, 1997.
        Attorney for licensee: N.S. Reynolds, Esquire, Winston & Strawn, 
    1400 L Street N.W., Washington, D.C. 20005-3502
        Local Public Document Room location:  University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        NRC Acting Project Director: James Clifford, Acting
        Dated at Rockville, Maryland, this 23rd day of July 1997.
        For The Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation
    [Doc. 97-19910 Filed 7-29-97; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
05/07/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-11910
Dates:
Immediately, to be implemented within 30 days.
Pages:
40843-40868 (26 pages)
PDF File:
97-11910.pdf