X97-10507. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 88 (Wednesday, May 7, 1997)]
    [Notices]
    [Pages 24984-24997]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X97-10507]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from April 12, 1997, through April 25, 1997. The 
    last biweekly notice was published on April 23, 1997 (62 FR 19825).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S.
    
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    Nuclear Regulatory Commission, Washington, DC 20555-0001, and should 
    cite the publication date and page number of this Federal Register 
    notice. Written comments may also be delivered to Room 6D22, Two White 
    Flint North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. 
    to 4:15 p.m. Federal workdays. Copies of written comments received may 
    be examined at the NRC Public Document Room, the Gelman Building, 2120 
    L Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By June 6, 1997, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley 
    Power Station, Unit No. 1, Shippingport, Pennsylvania
    
        Date of amendment request: March 10, 1997
        Description of amendment request: The proposed amendment would 
    modify the Technical Specifications (TSs) by reducing the reactor 
    coolant system (RCS) specific activity limits in accordance with 
    Generic Letter 95-05. The definition of DOSE EQUIVALENT I-131 would be 
    replaced with the Improved Standard TS definition wording in the first 
    sentence and an
    
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    equation added based on dose conversion factors derived from 
    International Commission on Radiation Protection (ICRP) ICRP-30. TS 
    3.4.8, Specific Activity, would be revised by reducing the DOSE 
    EQUIVALENT I-131 limit from 1.0 [micro]Ci[curies]/gram to 0.35 
    [micro]Ci[curies]/gram. Item 4.a in TS Table 4.4-12, Primary Coolant 
    Specific Activity Sample and Analysis Program, TS Figure 3.4-1, and the 
    Bases for TS 3/4.4.8 would be modified to reflect the reduced DOSE 
    EQUIVALENT I-131 limit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change reduces the reactor coolant system (RCS) 
    specific activity limits of Specification 3.4.8 from 1.0 [micro]Ci/
    gram to 0.35 [micro]Ci/gram and lowers the graph in Figure 3.4-1 by 
    39 [micro]/Ci gram following the guidance provided in Generic Letter 
    (GL) 95-05. This reduces the RCS activity allowed to leak to the 
    secondary side when the plant is operating so that additional margin 
    is available to support a higher allowable accident-induced leakage 
    value as justified by analysis.
        The proposed changes to Specification 3.4.8 and the definition 
    of DOSE EQUIVALENT I-131 ensure these requirements are consistent 
    the latest analyses.
        These changes implement the more restrictive RCS activity limits 
    in accordance with applicable analyses and GL 95-05 to ensure the 
    regulations are satisfied. Therefore, these changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not alter the configuration of the 
    plant or affect the operation with the reduced specific activity 
    limit. By reducing the specific activity limit, the limit would be 
    reached sooner to initiate evaluation of the out of limit condition. 
    The proposed changes will not result in any additional challenges to 
    the main steam system or the reactor coolant system pressure 
    boundary. Consequently, no new failure modes are introduced as a 
    result of the proposed changes. As a result, the main steam line 
    break, steam generator tube rupture and loss of coolant accident 
    analyses remain bounding. Therefore, the proposed change will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed change reduces the RCS specific activity limit to 
    0.35 [micro]Ci/gram along with lowering the Figure 3.4-1 limits by 
    39 [micro]Ci/gram. Reduction of the RCS specific activity limits 
    allows an increase in the limit for the projected SG [steam 
    generator] leakage following SG tube inspection and repair in 
    accordance with the voltage-based SG tube alternate repair criteria 
    (ARC) incorporated by Amendment No. 198. This follows the guidance 
    provided in GL 95-05 and effectively takes margin available in the 
    specific activity limits and applies it to the projected SG leakage 
    for the ARC. This has been determined to be an acceptable means for 
    accepting higher projected leakage rates while still meeting the 
    applicable limits of 10 CFR [Part] 100 and GDC [General Design 
    Criterion] 19 with respect to offsite and control room doses.
        The capability for monitoring the specific activity and 
    complying with the required actions remains unchanged. In addition, 
    there is no resultant change in dose consequences. Therefore, the 
    proposed change does not involve a significant reduction in a margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: March 14, 1997
        Description of amendment request: The proposed amendment would 
    relocate the following administrative control technical specifications 
    (TSs) from the Beaver Valley Power Station, Unit Nos. 1 and 2 (BVPS-1 
    and BVPS-2) TSs to the quality assurance program description, which is 
    presented in Section 17.2 of the BVPS-2 Updated Final Safety Analysis 
    Report (UFSAR). Section 17.2 of the BVPS-2 UFSAR contains the quality 
    assurance program description for both BVPS-1 and BVPS-2. The licensee 
    stated that the proposed changes are based on NRC Administrative Letter 
    95-06, ``Relocation of Technical Specification Administrative Controls 
    Related to Quality Assurance.''
        BVPS-2 TS 6.2.3 (Independent Safety Evaluation Group)
        BVPS-1 and BVPS-2 TS 6.5.1 (Onsite Safety Committee)
        BVPS-1 and BVPS-2 TS 6.5.2 (Offsite Review Committee)
        BVPS-1 and BVPS-2 TS 6.8.2 (Procedures, Review and Approval)
        BVPS-1 and BVPS-2 TS 6.8.3 (Temporary Procedure Changes, Review and 
    Approval)
        BVPS-1 and BVPS-2 TS 6.10.1 (Records Retention, At least 5 years)
        BVPS-1 and BVPS-2 TS 6.10.2 (Records Retention, Duration of 
    Operating License)
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        This proposed change would relocate technical specification 
    administrative controls to the quality assurance program 
    description. Adequate controls are provided by the established 
    quality assurance program change process in 10 CFR 50.54(a).
        The provisions of Technical Specification 6.2.3.2 which states 
    that: ``The ISEG [Independent Safety Evaluation Group] shall be 
    composed of at least five, dedicated, full-time engineers located on 
    site,'' would be omitted from the provisions relocated to the 
    quality assurance program description. Since no system, component or 
    operational procedure changes are involved, and the ISEG function 
    will continue to be implemented, the change can have no effect on 
    safe operation of the plant.
        The likelihood that an accident will occur is not increased by 
    this proposed technical specification change which involves 
    administrative controls. No systems, equipment, or components are 
    affected by the proposed change. Thus, the consequences of a 
    malfunction of equipment important to safety previously evaluated in 
    the Updated Final Safety Analysis Report (UFSAR) are not increased 
    by this change.
        Relocation of technical specification provisions and related 
    changes do not affect possible initiating events for accidents 
    previously evaluated or any system functional requirement. The 
    proposed changes have no impact on accident initiators or plant 
    equipment, and do not affect the probabilities or consequences of an 
    accident.
        Therefore, the proposed changes will not involve a significant 
    increase in the probability or consequences of a previously 
    evaluated accident.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed relocation of technical specification provisions to 
    the quality assurance program description and related changes do not 
    involve changes to the physical plant or operations. Since the 
    proposed changes to administrative controls do not affect equipment 
    or its operation, they cannot contribute to accident initiation and
    
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    cannot produce a new accident scenario or a new type of equipment 
    malfunction.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes are administrative in nature and do not 
    directly affect plant equipment or operation. Safety limits and 
    limiting safety system settings are not affected by this proposed 
    change. The proposed changes do not affect the UFSAR design bases, 
    accident assumptions, or technical specification bases. In addition, 
    the proposed changes do not affect release limits, monitoring 
    equipment or practices.
        Therefore, the proposed changes would not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: April 11, 1997
        Description of amendment request: The proposed amendment modifies 
    Technical Specification (TS) 3.3.3.7.3 and Surveillance Requirement 
    4.3.3.7.3 for the broad range gas detection system at Waterford Steam 
    Electric Station, Unit 3. The proposed change also includes changes in 
    TS Basis 3/4.3.3.7.3 to support the changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The broad range gas detection system has no effect on the 
    accidents analyzed in chapter 15 of the Final Safety Analysis 
    Report. It's only effect is on habitability of the control room, 
    which will be enhanced by installation of the new monitoring system 
    and this change to the Technical Specifications. Analysis has shown 
    that the impact on operator incapacitation and subsequent core 
    damage risk of this background check is negligible.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        The proposed Technical Specification change in itself does not 
    change the design or configuration of the plant. The new system for 
    broad range toxic gas monitoring performs the same function as the 
    old system, but it accomplishes this with a more sophisticated 
    system that increases reliability.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        The broad range gas detection system has no effect on a margin 
    of safety as defined by Section 2 of the Technical Specifications. 
    It's only effect is on habitability of the control room, which will 
    be enhanced by installation of the new monitoring system and this 
    change to the Technical Specifications.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of amendment request: April 10, 1997
        Description of amendment request: The proposed changes would modify 
    the Technical Specifications (TSs) for the Enclosure Building. The 
    Enclosure Building is a limited-leakage, steel-framed structure that 
    completely surrounds the containment. It is designed and constructed to 
    ensure that any leakage of radioactive materials to the environment 
    would not exceed an acceptable upper limit in the event of a design 
    basis loss-of-coolant accident or movement of loads over the spent fuel 
    pool. A slight negative pressure is maintained by the Enclosure 
    Building Filtration System and the system exhausts the filtered air 
    through charcoal and high-efficiency particulate air (HEPA) filters.
        Specifically, the proposed changes would relocate the surveillance 
    requirement for attaining a negative pressure in the Enclosure Building 
    from TS 3.6.5.1 ``Enclosure Building Filtration System,'' to TS 
    3.6.5.2, ``Enclosure Building Integrity.'' TS 3.6.5.2 would also be 
    changed to address operability, which includes integrity requirements, 
    and the Definition 1.25, ``Enclosure Building Integrity,'' would be 
    deleted. TS 4.6.5.2, ``Surveillance Requirements,'' would be modified 
    to require each access opening in the Enclosure Building to be closed 
    instead of the current requirement to close each door (some access 
    openings have two doors in series) in each access opening. This TS 
    would also be renumbered as 4.6.5.2.1.
        In addition, editorial changes are proposed for consistency and the 
    index pages would be updated to reflect the proposed changes. The TS 
    Bases would also be updated to reflect the proposed changes including 
    the need to maintain the integrity of the Enclosure Building and to 
    support previously approved laboratory testing requirements for 
    charcoal filter sample testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes to Technical Specifications 3.6.5.1 and 
    3.6.5.2, relocation of Surveillance Requirement 4.6.5.1.d.3 to 
    Specification 3.6.5.2, changes to Bases Sections 3.6.5.1 and 
    3.6.5.2, and deletion of Definition 1.25 will resolve the conflict 
    that currently exists between Specifications 3.6.5.1 and 3.6.5.2. 
    Specifically, the requirement to establish and maintain a negative 
    pressure in the Enclosure Building boundary included in 
    Specification 3.6.5.1 belongs in Specification 3.6.5.2. In the event 
    Enclosure Building operability is not maintained in Modes 1-4, the 
    Action Statement for LCO [limiting condition for operation] 3.6.5.2 
    requires that Enclosure Building operability must be restored within 
    24 hours. Twenty-four hours is a reasonable completion time 
    considering the limited leakage design of containment and the low
    
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    probability of a DBA [design-basis accident] occurring during this 
    time period. Therefore, it is considered that there exists no loss 
    of safety function. The
        proposed changes do no modify the LCO or surveillance acceptance 
    criterion, nor do they change the frequency of the surveillances. 
    The proposed changes do not involve any physical changes to the 
    plant, do not alter the way any structure, system, or component 
    functions. Therefore, the structures, systems, or components will 
    perform their intended function when called upon. (The redundancy of 
    the double doors has not been credited in the radiological dose 
    calculations for any Design Basis Accident.) Additionally, the 
    proposed changes are consistent with the new, improved Standard 
    Technical Specifications for Combustion Engineering plants (NUREG-
    1432).
        The editorial changes to Technical Specifications 3.6.5.1, 
    3.6.5.2, and 3.9.15 do not change any technical aspect of these 
    specifications. Therefore the proposed changes do not affect the 
    probability of any previously evaluated accident.
        Based on the above, the proposed changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes do not make any physical or operational 
    changes to existing plant structures, systems, or components. The 
    proposed changes do not introduce any new failure modes. The 
    proposed changes simply resolve a conflict which currently exits 
    between Specifications 3.6.5.1 and 3.6.5.2. Thus, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes do not have any adverse impact on the 
    accident analyses. Also, the proposed changes resolve a conflict 
    which currently exists between Specifications 3.6.5.1 and 3.6.5.2. 
    The structures, systems, or components covered under Specifications 
    3.6.5.1 and 3.6.5.2 will perform their intended safety function when 
    called upon.
        Based on the above, there is no significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Deputy Director: Phillip F. McKee
    
    PECO Energy Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Dockets Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station, Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: March 31, 1997
        Description of amendment request: The proposed change revises the 
    Peach Bottom Atomic Power Station, Units 2 and 3 technical 
    specifications to extend the surveillance interval for calibration of 
    Average Power Range Monitor (APRM) flow bias instrumentation from 18 
    months to 24 months.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the accidents previously evaluated take credit only for the 
    clamped 120% high neutron flux scram setpoint. Credit is not taken 
    for the flow biased APRM scram setpoint. Failure or inaccuracy of 
    the flow biased feature of the APRM scram setpoint will in no way 
    affect the clamped high flux scram setpoint. The 120% high flux 
    scram setpoint is derived internal to the APRM circuitry and 
    calibrated separately as part of the APRM trip circuitry. The APRM 
    clamped high flux scram setpoint is not being impacted by the 
    proposed changes and will be automatically enforced regardless of 
    the status or accuracy of the APRM flow bias circuitry.
        Because there is no impact on the clamped 120% high neutron flux 
    scram setpoint which is the only APRM scram setpoint with any 
    analytical safety basis, the proposed changes will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because the proposed changes do not allow plant operation in any 
    mode that is not already evaluated. The APRM system provides 
    monitoring and accident mitigation functions to limit peak flux in 
    the core during Modes 1 and 2. No pressure boundary interfaces or 
    process control parameters will be challenged in any way as to 
    create the possibility of a new or different type of accident than 
    any previously evaluated. Also, failure of the sensing line 
    associated with flow transmitters to measure recirculation drive 
    flow has already been accounted for in the initial plant design by 
    including excess flow check valves for sensing line break isolation. 
    Therefore, these changes will not create the possibility of a new or 
    different kind of accident than any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety because the APRM flow biased high flux scram 
    is not credited in the PBAPS safety analysis. Because the proposed 
    changes do not impact safety analysis assumptions, these proposed 
    changes will not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101
        NRC Project Director: John F. Stolz
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: April 22, 1997
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    Section 4.2.b, ``Steam Generator Tubes,'' to allow a laser-welded 
    repair of Westinghouse hybrid expansion joint (HEJ) sleeved steam 
    generator (SG) tubes. The proposed repair process would fuse the tube 
    to the sleeve in the upper joint of the existing HEJ sleeved tubes. The 
    repair weld would be made in either the hardroll (HR) expansion or the 
    upper hydraulic expansion (HE) region of the HEJ. By fusing the tube to 
    the sleeve, parent tube degradation below the weld would be isolated 
    and a new pressure boundary would be formed. The new pressure boundary 
    would satisfy both the structural and leakage integrity requirements of 
    the sleeved tube assembly with no change in the flow or heat transfer 
    characteristics of the sleeved tube. The proposed amendment supersedes 
    in its entirety a previously submitted proposed amendment dated 
    September 6, 1996, which was noticed in the Federal Register on October 
    15, 1996 (61 FR 53769).
    
    [[Page 24989]]
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the KNPP in accordance with the proposed license 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The laser-weld repair of HEJ sleeved tubes in either the HR or 
    HE location will not affect the tube, sleeve, or weld stress 
    conditions or fatigue usage factors such that the limits of the ASME 
    Boiler and Pressure Vessel Code are exceeded. Accelerated corrosion 
    testing performed on prototypic HR welds, and a corrosion assessment 
    performed for the HE welds concluded that the repair welds will not 
    result in aggravated stress corrosion cracking at the weld-repair 
    location. Any postulated sleeve joint degradation would occur at a 
    relatively slow rate and would be detectable by routine non-
    destructive examination (NDE) inspection prior to reaching any 
    applicable safety margins. Therefore, use of the laser-weld repair 
    process will not result in an increased probability of an accident 
    previously evaluated.
        A post-weld stress relief ultrasonic test inspection is required 
    to verify minimum acceptable weld thickness to ensure that the weld 
    stresses do not exceed ASME Code limits for both stress intensity 
    and fatigue usage. Leakage testing of laser-welded sleeve joints, 
    and in-situ leakage testing of the laser-welded repairs (LWR) at 
    KNPP, demonstrate a leak-tight joint at pressures up to main steam 
    line break. Mechanical testing of 7/8 inch laser-welded tubesheet 
    sleeves installed in roll-expanded tubes has shown that the 
    individual joint structural strength of Alloy 690 laser-welded 
    sleeves under normal, upset, and faulted conditions provides margin 
    to acceptable limits. These acceptable limits bound the most 
    limiting (3 times normal operating pressure differential) 
    recommended by Regulatory Guide (RG) 1.121.
        The HEJ sleeve plugging limit currently defined in the TS is 
    reduced from 31% to 24% throughwall due to the use of ASME code 
    minimum material properties values for the sleeve material. Minimum 
    wall thickness requirements (used for developing the depth-based 
    plugging limit for the sleeve) are determined using the guidance of 
    RG 1.121 and the pressure stress equation of Section 3 of the ASME 
    Code.
        The hypothetical consequences of failure of the laser-welded 
    repaired HEJ would be bounded by the current SG tube rupture (SGTR) 
    analysis covered in the KNPP Updated Safety Analysis Report. Due to 
    the slight reduction in diameter caused by the sleeve wall 
    thickness, primary coolant release rates would be slightly less than 
    assumed for the SGTR, and, therefore, would result in lower primary 
    fluid mass release to the secondary system. The laser-weld repair 
    process does not change the existing reactor coolant system flow 
    conditions; therefore, existing loss of coolant accident (LOCA) and 
    non-LOCA analysis results will be unaffected. Plant response to 
    design basis accidents for the current tube plugging and flow 
    conditions are not affected by the repair process; no new tube 
    diameter restrictions are introduced. Therefore, the application of 
    the repair weld will not increase the consequences of a previously 
    evaluated accident.
        2. The proposed license amendment request does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Application of laser-welded repair for the HEJ sleeved tubes 
    will not introduce significant or adverse changes to the plant 
    design basis. The general configuration of the HEJ sleeve is 
    unaffected by the repair process. The repair process also does not 
    represent a potential to affect any other plant component. Stress 
    and fatigue analysis of the repair has shown that the ASME Code and 
    RG 1.121 criteria are not exceeded. Application of the laser-weld 
    repair to the HEJ sleeved tubes maintains overall tube bundle 
    structural and leakage integrity. Extensive testing and evaluation 
    including examination of actual pulled tube samples verified 
    adequate structural and leakage integrity of repair HEJs, which had 
    acceptable NDE.
        Any hypothetical accident as a result of potential tube or 
    sleeve degradation in the repaired portion of the joint is bounded 
    by the existing tube rupture accident analysis. Therefore, use of 
    the laser-welded repair process will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in the margin of safety.
        The laser-weld repair of the HEJ sleeved tubes has been shown to 
    restore integrity of the tube bundle consistent with its original 
    design basis conditions; i.e., tube/sleeve operational and faulted 
    load stresses and cumulative fatigue usage factors are bounded by 
    ASME Code requirements and the tubes are leak tight under all plant 
    conditions. Based on the results of the structural and leakage 
    testing performed on LWR joints pulled from the KNPP SGs and 
    supporting analytical evaluations, application of laser-welded 
    repair will not result in a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P.O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: Gail H. Marcus
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: April 24, 1997
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    Section 4.2.b, ``Steam Generator Tubes,'' to allow repair of steam 
    generator (SG) tubes with Combustion Engineering (CE) leak-tight 
    sleeves in accordance with CE generic topical report CEN-629-P, 
    Revision 2, ``Repair of Westinghouse Series 44 and 51 Steam Generator 
    Tubes Using Leak-Tight Sleeves.'' The TS would also be revised to allow 
    re-sleeving of tubes with existing sleeve joints in accordance with 
    KNPP specific topical report CEN-632-P, ``Repair of Kewaunee Steam 
    Generator Tubes Using a Re-Sleeving Technique.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the KNPP in accordance with the proposed license 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The supporting technical evaluation and safety evaluation for 
    the CE leak-tight sleeves demonstrates that the sleeve configuration 
    will provide SG tube structural and leakage integrity under normal 
    operating and accident conditions. The sleeve configurations have 
    been designed and analyzed in accordance with the requirements of 
    the ASME Code. Mechanical testing has shown that the sleeve and 
    sleeve joints provide margin above acceptance limits. Ultrasonic 
    testing is used to verify the leak tightness of the weld above the 
    tubesheet. Testing has demonstrated the leak tightness of the 
    hardroll joint as well as the structural integrity of the hardroll 
    joint. Tube rupture cannot occur at the hardroll joint due to the 
    reinforcing effect of the tubesheet. Tests have demonstrated that 
    tube collapse will not occur due to postulated loss of coolant 
    accident loadings.
        The existing TS leak-rate requirements and accident analysis 
    assumptions remain unchanged in the event that significant leakage 
    does occur from the sleeve joint or the sleeve assembly ruptures. 
    Any leakage through the sleeve assembly is fully bounded by the 
    existing SG tube rupture analysis included in the KNPP Updated Final 
    Safety Analysis Report. The proposed sleeving and re-sleeve repair 
    processes do not adversely impact any other previously evaluated 
    design basis accidents.
        2. The proposed license amendment request does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
    
    [[Page 24990]]
    
        Installation of the sleeves or re-sleeves does not introduce any 
    significant changes to the plant design basis. The use of a sleeve 
    to span the area of degradation of the SG tube restores the 
    structural and leakage integrity of the tubing to meet the original 
    design basis. Stress and fatigue analysis of the sleeve assembly 
    shows that the requirements of the ASME Code are met. Mechanical 
    testing has demonstrated that margin exists above the design 
    criteria. Any hypothetical accident as a result of any degradation 
    in the sleeved tube would be bounded by the existing tube rupture 
    accident analysis.
        3. The proposed license amendment does not involve a significant 
    reduction in the margin of safety.
        The use of sleeves to repair degraded SG tubing has been 
    demonstrated to maintain the integrity of the tube bundle 
    commensurate with the requirements of the ASME Code and draft 
    Regulatory Guide 1.121, and to maintain the primary to secondary 
    pressure boundary under normal and postulated accident conditions. 
    The safety factors used in the verification of the strength of the 
    sleeve assembly are consistent with the safety factors in the ASME 
    Boiler and Pressure Vessel Code used in SG design. The operational 
    and faulted condition stresses and cumulative usage factors are 
    bounded by the ASME Code requirements. The sleeve assembly has been 
    verified by testing to prevent both tube pullout and significant 
    leakage during normal and postulated accident conditions. A test 
    program was conducted to ensure the lower hardrolled joint design 
    was leak tight and capable of withstanding the design loads. The 
    primary coolant pressure boundary of the sleeve assembly will be 
    periodically inspected by non-destructive examination to identify 
    sleeve degradation due to operation.
        Installation of the sleeves and re-sleeves will decrease the 
    number of tubes that must be taken out-of-service due to plugging. 
    There is a small amount of primary coolant flow reduction due to the 
    sleeve for which an equivalent plugging sleeve to plug ratio is 
    assigned based on sleeve length. The ratio is used to assess the 
    final equivalent plugging percentage as an input to other safety 
    analyses. Because the sleeve maintains the design basis requirements 
    for the SG tubing, it is concluded that the proposed change does not 
    result in a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P.O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: Gail H. Marcus
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Elecric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: March 27, 1997
        Brief description of amendments: The proposed amendments would 
    revise the Technical Specifications for the Brunswick Steam Electric 
    Plant Units 1 and 2 to eliminate certain instrumentation response time 
    testing requirements in accordance with NRC-approved BWR Owners Group 
    Topical Report NEDO-32291-A, ``System Analysis for the Elimination of 
    Selected Response Time Testing Requirements.''
        Date of publication of individual notice in Federal Register: April 
    1, 1997(62 FR 15542)
        Expiration date of individual notice: May 1, 1997
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota, and Docket No. 50-263, Monticello Nuclear 
    Generating Plant, Wright County, Minnesota
    
        Date of amendment requests: December 6, 1996
        Description of amendment requests: The licensee requests amendments 
    to the Prairie Island and Monticello operating licenses to reflect the 
    Commission's approval of the transfer of control over the subject NRC 
    licenses held by Northern States Power Company (NSP). On October 20, 
    1995, as supplemented August 28, 1996, NSP requested NRC approval for 
    the transfer of control of licenses. The Commission is considering the 
    issuance of amendments to the licenses to reflect the above transfer 
    approved by the Commission on April 1, 1997 (62 FR 17882, dated April 
    11, 1997).
        Date of individual notice in the Federal Register: April 11, 1997 
    (62 FR 17882)
        Expiration date of individual notice: May 12, 1997
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: April 4, 1997
        Brief description of amendment request: The proposed amendment 
    would clarify the scope of the surveillance requirements for response 
    time testing of instrumentation in the reactor protection system, 
    isolation actuation system, and emergency core cooling system in the 
    Technical Specifications for each unit (Sections 4.3.1.3, 4.3.2.3, and 
    4.3.3.3).
        Date of publication of individual notice in Federal Register: April 
    17, 1997 (62 FR 17885)
        Expiration date of individual notice: May 19, 1997
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant
    
    [[Page 24991]]
    
    Hazards Consideration Determination, and Opportunity for A Hearing in 
    connection with these actions was published in the Federal Register as 
    indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved. Boston Edison Company, Docket No. 
    50-293, Pilgrim Nuclear Power Station, Plymouth County, Massachusetts
        Date of application for amendment: January 24, 1997, as 
    supplemented March 27, 1997
        Brief description of amendment: The proposed amendment will update 
    the Safety Limit Minimum Critical Power Ratio (SLMCPR) in Technical 
    Specification 2.1.2 and the associated Bases section to reflect the 
    results of the latest cycle-specific calculation performed for the 
    Pilgrim Nuclear Power Station Operating Cycle 12. In addition, the 
    values provided in Note 5 of Table 3.2.C.1, which are based on the 
    SLMCPR values, have been revised as a result of the changes to the 
    SLMCPR value.
        Date of issuance: April 7, 1997
        Effective date: April 7, 1997
        Amendment No.: 171
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6568) The March 27, 1997, supplemental letter provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated April 7, 1997 No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of application for amendment: March 27, 1997, as supplemented 
    April 11, 1997.
        Brief description of amendment: The amendments revise the Technical 
    Specifications relating to response time testing requirements 
    associated with the reactor protection system, isolation system, and 
    emergency core cooling system.
        Date of issuance: April 18, 1997
        Effective date: April 18, 1997
        Amendment Nos.: 184 and 215
        Facility Operating License Nos. DPR-71 and DPR-62. Amendments 
    revised the Technical Specifications. Public comments requested as to 
    proposed no significant hazards consideration (NSHC): Yes (62 FR 15542 
    dated April 1, 1997). The notice provided an opportunity to submit 
    comments on the Commission's proposed NSHC determination. No comments 
    have been received. The notice also provided for an opportunity to 
    request a hearing by May 1, 1997, but indicated that if the Commission 
    makes a final NSHC determination, any such hearing would take place 
    after issuance of the amendments. The Commission's related evaluation 
    of the amendment, finding of exigent circumstances, and final 
    determination of NSHC are contained in a Safety Evaluation dated April 
    18, 1997.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: December 21, 1995, as 
    supplemented on October 24, 1996, and March 24, 1997.
        Brief description of amendments: The amendments relocate certain 
    cycle-specific parameter limits from the Technical Specifications (TS) 
    to the Operating Limits Report. The cycle-specific parameter limits to 
    be relocated are for Shutdown Rod Insertion Limit, Control Rod 
    Insertion Limits, Axial Flux Difference Target Band, Heat Flux Hot 
    Channel Factor [FQ(z)], and Nuclear Enthalpy Rise Hot 
    Channel Factor (FN delta H). In addition, your March 24, 
    1997, submittal contained supplementary revisions to the Bases section 
    associated with the above TS change. The supplementary Bases pages will 
    be reviewed and transmitted to you under separate cover. Finally, 
    Braidwood's TS 6.9.1.7 title was corrected.
        Date of issuance: April 16, 1997
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 88, 88, 80, 80
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 20, 1997 (62 
    FR 7804). The March 24, 1997, submittal provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated April 16, 1997. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: April 29, 1996, as supplemented 
    on January 21 and March 25, 1997.
        Brief description of amendments: The amendments would: (1) revise 
    Technical Specification (TS) 3.7.1.1, Action a., to require the unit to 
    be in hot shutdown, rather than cold shutdown, for consistency with 
    NUREG-1431, ``Standard Technical Specifications for Westinghouse 
    Plants,'' and add a new Action b. to clarify the shutdown requirements 
    when there are more than three inoperable main steam line American 
    Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code 
    (Code) safety valves on any
    
    [[Page 24992]]
    
    one steam generator; (2) revise TS Surveillance Requirement 4.7.1.1 to 
    clarify that Specification 4.0.4 does not apply for entry into Mode 3 
    for Byron and Braidwood and for Braidwood only, delete the one-time 
    requirements for Unit 1, Cycle 5 and Unit 2 after outage A2F27; (3) 
    revise the maximum allowable power range neutron flux high trip 
    setpoints in Table 3.7-1; (4) revise Table 3.7-2 to increase the as-
    found main steam safety valve (MSSV) lift setpoint tolerance to plus or 
    minus 3 percent, provide an as-left setpoint tolerance of plus or minus 
    1 percent, and change a table notation; (5) delete the orifice size 
    column from Table 3.7-2; and (6) revise the Bases for TS 3.7.1.1 to be 
    consistent with the proposed changes to TS 3.7.1.1.
        Date of issuance: April 15, 1997
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 87, 87, 79, and 79
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: March 12, 1997 (62 FR 
    11486). The March 25, 1997, submittal provided additional information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated April 15, 1997. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: August 7, 1996, as supplemented 
    March 12, 1997.
        Brief description of amendment: The amendment revises Technical 
    Specifications to allow the use of 10 CFR Part 50, Appendix J, Option 
    B, ``Performance-Based Containment Leak Rate Testing.''
        Date of issuance: April 10, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 190
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 11, 1996 (61 
    FR 47976) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 10, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of application for amendment: March 27, 1997, as supplemented 
    on April 4, 1997
        Brief description of amendment: The amendment revises technical 
    specification surveillance requirement (SR) 4.3.1.3 for the Reactor 
    Protection System Instrumentation to indicate that certain sensors are 
    exempt from response time testing. A similar revision is made to SR 
    4.3.2.3 for the Isolation Actuation Instrumentation. Finally, SR 
    4.3.3.3 for the Emergency Core Cooling System Actuation Instrumentation 
    is revised to indicate that the emergency core cooling system actuation 
    instrumentation is exempt from response time testing.
        Date of issuance: April 18, 1997
        Effective date: April 18, 1997, with full implementation prior to 
    entry into Operation Condition 2 or 3
        Amendment No.: 111
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    considerations (NSHC): Yes (62 FR 15731 dated April 2, 1997). The 
    notice provided an opportunity to submit comments on the Commission's 
    proposed NSHC determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by May 2, 1997, 
    but indicated that if the Commission makes a final NSHC determination, 
    any such hearing would take place after issuance of the amendment. The 
    Commission's related evaluation of the amendment, finding of exigent 
    circumstances, and final determination of NSHC are contained in a 
    Safety Evaluation dated April 18, 1997.
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina Date of 
    application for amendments: January 6, 1997, as supplemented by 
    letters dated April 10 and 15, 1997
    
        Brief description of amendments: The amendments revise portions of 
    the Technical Specifications to permit a one-time operation of the 
    Containment Purge Ventilation System during Modes 3 and 4 after the 
    current and forthcoming steam generator replacement outages.
        Date of issuance: April 24, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 174 and 156
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6574) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 24, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, North Carolina 28223-0001
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments: September 9, 1996
        Brief description of amendments: These amendments modify the design 
    features section (Section 5.0) of the Technical Specifications (TSs) to 
    make the design features section consistent with the intent of 10 CFR 
    50.36 and with the guidance provided in the NRC's Standard Technical 
    Specifications, Westinghouse Plants (NUREG-1431, Revision 1).
        Date of issuance: April 14, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 202 and 83
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64384) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated April 14, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library,
    
    [[Page 24993]]
    
    663 Franklin Avenue, Aliquippa, PA 15001
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: December 19, 1996
        Brief description of amendment: The amendment deletes the specific 
    value for the total reactor coolant system volume from the Design 
    Features section of the Technical Specifications.
        Date of issuance: April 16, 1997
        Effective date: April 16, 1997
        Amendment No.: 181
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4348) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 16, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of application for amendment: December 19, 1996
        Brief description of amendment: Request to add CENTS code as a 
    Reference to the Technical Manual used for determining Core Operating 
    Limits Report in the Technical Specifications.
        Date of issuance: April 24, 1997
        Effective date: April 24, 1997
        Amendment No.: 182
        Facility Operating License No. NPF-6: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4347) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 24, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: January 10, 1997
        Brief description of amendment: The amendment revises the technical 
    specifications for reactor pressure vessel pressure and temperature 
    limits by providing new limits that are valid to 12 effective full 
    power years.
        Date of issuance: April 14, 1997
        Effective date: April 14, 1997
        Amendment No.: 93
        Facility Operating License No. NPF-47: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8798) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 14, 1997. No significant 
    hazards consideration comments received. No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: November 7, 1995, as supplemented by 
    letters dated July 17, and December 26, 1996, and February 27, March 
    14, April 7, and April 17, 1997.
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications by revising TS 3/4.8.1, ``Electrical Power 
    Systems - A.C. Sources,'' to incorporate recommendations and 
    suggestions from (1) Generic Letter (GL) 93-05, ``Line-Item Technical 
    Specifications Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operations;'' (2) GL 94-01, ``Removal of 
    Accelerated Testing and Special Reporting Requirements for Emergency 
    Diesel Generators from Plant Technical Specifications;'' and (3) NUREG-
    1432, ``Standard Technical Specifications Combustion Engineering 
    Plants.''
        Date of issuance: April 21, 1997
        Effective date: April 21, 1997, to be implemented within 60-days.
        Amendment No.: 126
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    180) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated April 21, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: October 10, 1996 (TSCR 243)
        Brief description of amendment: The amendment modifies the 
    Technical Specifications (TS) by replacing the description of the 
    existing permissive interlock from AC Voltage to Core Spray Booster 
    Pump d/p Permissive:  21.2 psid for initiation of the 
    automatic depressurization system, adds corresponding surveillance 
    requirements, and adds notes clarifying functional requirements.
        Date of Issuance: April 14, 1997
        Effective date: April 14, 1997, with full implementation within 60 
    days
        Amendment No.: 190
        Facility Operating License No. DPR-16.
        Date of initial notice in Federal Register: November 6, 1996 (61 FR 
    57485). The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated April 14, 1997 No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: September 5, 1996
        Brief description of amendment: The amendment deletes License 
    Condition 2.C.(5), ``Integrated Implementation Schedule'' from the 
    Millstone Unit 1 Operating License.
        Date of issuance: April 15, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 100
        Facility Operating License No. DPR-21: Amendment revised the 
    Operating License.
        Date of initial notice in Federal Register: October 23, 1996 (61 FR 
    55036) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 15, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360 and at the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: February 5, 1996
    
    [[Page 24994]]
    
        Brief description of amendment: The amendment deletes a clause from 
    Technical Specification 4.0.5.a. Specifically, this change deletes the 
    clause ``(g), except where specific written relief has been granted by 
    the Commission pursuant to 10 CFR Part 50, Section 50.55a(g)(6)(i).'' 
    The amendment also makes the appropriate changes to the Bases section.
        Date of issuance: April 21, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 138
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8800) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 21, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: March 4, 1996
        Brief description of amendment: The amendment modifies Surveillance 
    Requirements 4.8.1.1.2.a.6, 4.8.1.1.2.b, and 4.8.1.1.2.g.7 by 
    specifying load bands in loading the diesel generator (DG) in lieu of 
    the present requirement to load the DG greater than or equal to a given 
    value. A footnote is being added to the three surveillance 
    rerquirements to indicate that a momentary transient outside the load 
    range shall not invalidate the test. The aassociated Bases sections 
    have been revised to reflect the above changes.
        Date of issuance: April 15, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 137
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 12, 1997 (62 FR 
    11496) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 15, 1997. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: February 14, 1996, as 
    supplemented by letter dated February 24, 1997.
        Brief description of amendments: The amendments revised the 
    combined Technical Specifications (TS) for the Diablo Canyon Power 
    Plant (DCPP) Unit Nos. 1 and 2 to revise 30 TS and add two new TS 
    surveillance requirements to support implementation of extended fuel 
    cycles at DCPP Unit Nos. 1 and 2. The specific TS changes include those 
    for 9 trip actuating device tests, 12 fluid system actuation tests, and 
    11 miscellaneous tests. Two of the fluid system actuation tests are new 
    TS surveillance requirements. The TS changes also involve adding a new 
    frequency notation, ``R24, REFUELING INTERVAL,'' to Table 1.1 of the 
    TS. Also, a revision that applies to all subsequent TS changes involves 
    revising the Bases Section of TS 4.0.2 to change the surveillance 
    frequency from an 18-month surveillance interval to at least once each 
    refueling interval.
        Date of issuance: April 14, 1997
        Effective date: April 14, 1997, to be implemented within 90 days 
    from the date of issuance.
        Amendment Nos.: Unit 1 - 118; Unit 2 - 116
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31183) The February 24, 1997, supplemental letter provided additional 
    clarifying information and did not change the staff's initial no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated April 14, 1997. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: May 31, 1996, as supplemented 
    by letter dated December 16, 1996.
        Brief description of amendments: The amendments revised the 
    combined Technical Specifications (TS) for the Diablo Canyon Power 
    Plant (DCPP) Unit Nos. 1 and 2 to revise 23 TS surveillance frequencies 
    from at least once every 18 months to at least once per refueling 
    outage (nominally 24 months) and to make administrative changes for 6 
    other TS to maintain consistency for TS that are not proposed for 
    surveillance extension. The specific TS changes proposed include those 
    for 2 response time tests, 3 containment spray system tests, and 24 
    ventilation system tests.
        Date of issuance: April 14, 1997
        Effective date: April 14, 1997, to be implemented within 90 days of 
    issuance.
        Amendment Nos.: Unit 1 - 119; Unit 2 - Amendment No. 117
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 9, 1996 (61 FR 
    52966) The December 16, 1996, supplemental letter provided additional 
    clarifying information and did not change the staffs initial no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated April 14, 1997. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: November 22, 1996
        Brief description of amendment: The amendment allows an increase in 
    the U-235 enrichment of fuel stored in the fresh fuel storage racks or 
    the spent fuel storage racks from 4.5 weight percent (w/o) U-235 to 5.0 
    w/o U-235.
        Date of issuance: April 15, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
    
    [[Page 24995]]
    
        Amendment No.: 173
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 15, 1997 (62 FR 
    2182) The Commission's related evaluation of the amendment is contained 
    in the Safety Evaluation dated April 15, 1997, and an Environmental 
    Assessment dated March 25, 1997. No significant hazards consideration 
    comments received: Yes
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket No. 50-366, Edwin I. Hatch 
    Nuclear Plant, Unit 2, Appling County, Georgia
    
        Date of application for amendments: December 3, 1996, as 
    supplemented by letters dated January 27 and April 4, 1997
        Brief description of amendments: The amendments revise Technical 
    Specification 2.1.1.2 to change the Safety Limit Minimum Critical Power 
    Ratio based on the cycle-specific analyses of Cycle 13 of a non-
    equilibrium core of all General Electric (GE) 9 fuel with varying 
    enrichments and Cycle 14 of a non-equilibrium mixed core of GE13 and 
    GE9 fuel.
        Date of issuance: April 17, 1997
        Effective date: For Cycle 13, as of the date of issuance; For Cycle 
    14, effective upon startup.
        Amendment Nos.: 148 for Cycle 13; 149 for Cycle 14
        Facility Operating License Nos. DPR-57 and NPF-5. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4349) The January 27 and April 4, 1997, letters provided additional 
    information that did not change the scope of the December 3, 1996, 
    application and the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated April 17, 1997. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: April 4, 1996, as supplemented 
    by letters dated January 10, February 7, February 13, March 17, March 
    19, March 20, March 25, April 1, April 6, April 10, April 11, and April 
    18, 1997.
        Brief description of amendments: The amendments revise the Sequoyah 
    Technical Specifications (TSs) and associated Bases to allow for the 
    conversion from Westinghouse fuel to Framatome Cogema Fuel, designated 
    Mark-BW. The planned fuel conversion begin with fuel cycle 9 for each 
    unit. The amendments would revise the TSs to reflect the fuel design 
    and vendor change. The licensee's evaluation was contained in Topical 
    Report BAW-10220P, ``Mark-BW Fuel Assembly Application for Sequoyah 
    Nuclear Units 1 and 2.''
        Date of issuance: April 21, 1997
        Effective date: As of the date of issuance to be implemented no 
    later than 45 days of its issuance for Unit 1, and implemented upon 
    installation of Framatome Cogema Fuel in the Unit 2 reactor vessel for 
    Unit 2.
        Amendment Nos.: 223 and 214
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the Technical Specifications and License Conditions.
        Date of initial notice in Federal Register: May 8, 1996 (61 FR 
    20856) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 21, 1997 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the
    
    [[Page 24996]]
    
    documents related to this action. Accordingly, the amendments have been 
    issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By June 6, 1997, the licensee 
    may file a request for a hearing with respect to issuance of the 
    amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342 6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Unit Nos. 2 and 3, Grundy County, Illinois
    
        Date of application for amendments: April 14, 1997, as supplemented 
    on April 17, April 22, and April 24, 1997.
        Brief description of amendments: The proposed amendments requested 
    (1) review and approval of an Unreviewed Safety Question (USQ) 
    involving the control room operator dose resulting from an error in the 
    secondary containment volume, (2) a change in Technical Specification 
    (TS) Surveillance Requirements (SR) 4.7. P.2.b and 4.7. P.3 values for 
    the allowed methyl iodide penetration for the standby gas treatment 
    charcoal adsorbers, and (3) change of TS 5.2.C to
    
    [[Page 24997]]
    
    reflect the new calculated free volume of the secondary containment. 
    The April 17, April 22 and April 24, 1997, submittals provided 
    additional clarifying information that did not change the initial 
    proposed no significant hazards consideration determination.
        Date of Issuance: April 25, 1997
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 158 and 153
        Facility Operating License Nos. DPR-19 and DPR-25: The amendments 
    revised the Technical Specifications. Press release issued requesting 
    comments as to proposed no significant hazards consideration: Yes. 
    April 22, 1997. Joliet Herald News. Comments received: No. The 
    Commission's related evaluation of the amendments, finding of exigent 
    circumstances, consultation with the State of Illinois and final 
    determination of no significant hazards consideration are contained in 
    a Safety Evaluation dated April 25, 1997.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450
        NRC Project Director: Robert A. Capra
    
    Pennsylvania Power and Light Company, Docket No. 50-388, 
    Susquehanna Steam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendment: April 16, 1997, and as 
    supplemented by a letter dated April 18, 1997
        Brief description of amendment: This amendment changes the footnote 
    in the Design Features Section 5.3.1 of the Technical Specifications to 
    allow the use of ATRIUM-10 fuel in Operational Conditions 3 and 4.
        Date of issuance: April 25, 1997
        Effective date: As of the date of issuance to be implemented upon 
    receipt.
        Amendment No.: 138
        Facility Operating License No. NPF-22: This amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes. The NRC published a public 
    notice of the proposed amendment, issued a proposed finding of no 
    significant hazards consideration and reqeusted that any comments on 
    the proposed no significant hazards consideration be provided to the 
    staff by the close of business on April 24, 1997. The notice was 
    published in the Wilkes-Barre Times Leader and the Berwick Press 
    Enterprise on April 22-24, 1997. Public comments were received and have 
    been addressed in the staff's safety evaluation.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultation with the State of Pennsylvania and 
    final no significant hazards consideration determination are contained 
    in a Safety Evaluation dated April 25, 1997.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
        Dated at Rockville, Maryland, this 30th day of April 1997.
        For the Nuclear Regulatory Commission
    Elinor G. Adensam,
    Deputy Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation.
    [Doc. 97-11725 Filed 5-6-97; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Effective Date:
4/7/1997
Published:
05/07/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X97-10507
Dates:
April 7, 1997
Pages:
24984-24997 (14 pages)
PDF File:
x97-10507.pdf